IR 05000250/2012005: Difference between revisions
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==Dear Mr. Nazar:== | ==Dear Mr. Nazar:== | ||
On December 31, 2012, the US Nuclear Regulatory Commission (NRC) completed an inspection at your Turkey Point Nuclear Plant Units 3 and 4. The enclosed integrated inspection report documents the inspection findings, which were discussed on January 16, 2013, with Mr. Kiley and other members of your staff. | On December 31, 2012, the US Nuclear Regulatory Commission (NRC) completed an inspection at your Turkey Point Nuclear Plant Units 3 and 4. The enclosed integrated inspection report documents the inspection findings, which were discussed on January 16, 2013, with Mr. | ||
Kiley and other members of your staff. | |||
The inspection examined activities conducted under your license as they relate to safety and compliance with the Commission's rules and regulations and with the conditions of your license. | The inspection examined activities conducted under your license as they relate to safety and compliance with the Commission's rules and regulations and with the conditions of your license. | ||
The inspectors reviewed selected procedures and records, observed activities, and interviewed personnel. One self-revealing finding of very low safety significance (Green) was identified during this inspection. This finding did not involve a violation of NRC regulatory requirements. | The inspectors reviewed selected procedures and records, observed activities, and interviewed personnel. | ||
One self-revealing finding of very low safety significance (Green) was identified during this inspection. This finding did not involve a violation of NRC regulatory requirements. | |||
If you disagree with a cross-cutting aspect assignment in this report, you should provide a response within 30 days of the date of this report, with the basis of your disagreement, to the Regional Administrator, Region II and the NRC Resident Inspector at Turkey Point Nuclear Plant. In accordance with 10 CFR 2.790 of the NRC's "Rules of Practice", a copy of this letter, its enclosure, and your response (if any) will be available electronically for public inspection in the NRC Public Document Room or from the Publicly Available Records (PARS) component of NRC's document system (ADAMS). ADAMS is accessible from the NRC Website at http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room). | If you disagree with a cross-cutting aspect assignment in this report, you should provide a response within 30 days of the date of this report, with the basis of your disagreement, to the Regional Administrator, Region II and the NRC Resident Inspector at Turkey Point Nuclear Plant. In accordance with 10 CFR 2.790 of the NRC's "Rules of Practice", a copy of this letter, its enclosure, and your response (if any) will be available electronically for public inspection in the NRC Public Document Room or from the Publicly Available Records (PARS) component of NRC's document system (ADAMS). ADAMS is accessible from the NRC Website at http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room). | ||
Sincerely,/RA/ Shane Sandal, Acting Chief Reactor Projects Branch 3 Division of Reactor Projects Docket Nos: 50-250, 50-251 License Nos: DPR-31, DPR-41 | Sincerely,/RA/ Shane Sandal, Acting Chief Reactor Projects Branch 3 Division of Reactor Projects | ||
Docket Nos: 50-250, 50-251 License Nos: DPR-31, DPR-41 | |||
===Enclosure:=== | ===Enclosure:=== | ||
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===w/Attachment:=== | ===w/Attachment:=== | ||
Supplemental Information cc w/encl: (See page 3) | Supplemental Information cc w/encl: (See page 3) | ||
_________________________ X SUNSI REVIEW COMPLETE G FORM 665 ATTACHED OFFICE RII:DRP RII:DRP RII:DRS RII:DRS RII:DRP RII:DRS RII:DRS RII:DRS SIGNATURE Via email Via email Via email Via email Via email Via email Via email Via email NAME JStewart THoeg PCapehart CFletcher MBarillas AVargas MCoursey WPursley DATE 01/22/2013 01/23/2013 01/22/2013 01/22/2013 01/22/2013 01/23/2013 01/22/2013 01/22/2013 E-MAIL COPY? YES NO YES NO YES NO YES NO YES NO YES NO YES NO YES NO OFFICE RII:DRS RII:DRS NRR RII:DRS NRR RII:DRP RII:DRP SIGNATURE Via email Via email Via email via email /BRB for/ Via email MJR /RA/ SRS /RA/ NAME RTaylor DMas AZoulis GKuzo JLaughlin MRiches SSandal DATE 01/22/2013 01/22/2013 01/22/2013 01/23/2013 01/28/2013 01/28/2013 01/30/2013 E-MAIL COPY? YES NO YES NO YES NO YES NO YES NO YES NO 3 | |||
cc w/encl: | |||
Alison Brown Nuclear Licensing | |||
Florida Power & Light Company Electronic Mail Distribution | |||
Larry Nicholson Director Licensing | |||
Florida Power & Light Company Electronic Mail Distribution | |||
Michael Kiley Site Vice President | |||
Turkey Point Nuclear Plant Florida Power and Light Company Electronic Mail Distribution Niel Batista Emergency Management Coordinator Department of Emergency Management and Homeland Security Electronic Mail Distribution Paul Freeman Vice President Organizational Effectiveness | |||
Florida Power & Light Company Electronic Mail Distribution | |||
Peter Wells Vice President | |||
Outage Support CFAM | |||
Florida Power & Light Company Electronic Mail Distribution | |||
Robert J. Tomonto Licensing Manager | |||
Turkey Point Nuclear Plant Florida Power & Light Company Electronic Mail Distribution | |||
Eric McCartney | |||
Plant General Manager | |||
Turkey Point Nuclear Plant Florida Power and Light Company Electronic Mail Distribution | |||
Cynthia Becker (Acting) Chief Florida Bureau of Radiation Control Department of Health Electronic Mail Distribution | |||
Attorney General Department of Legal Affairs The Capitol PL-01 Tallahassee, FL 32399-1050 | |||
James Petro Managing Attorney-Nuclear Florida Power & Light Company Electronic Mail Distribution | |||
County Manager of Miami-Dade County 111 NW 1st Street, 29th Floor Miami, FL 33128 | |||
George Gretsas City Manager City of Homestead Electronic Mail Distribution 4 | |||
Letter to Mano Nazar from Shane Sandal dated January 30, 2013 | |||
SUBJECT: TURKEY POINT NUCLEAR PLANT - NRC INTEGRATED INSPECTION REPORT 05000250/2012005 AND 05000251/2012005 | |||
Distribution w/encl | |||
: C. Evans, RII L. Douglas, RII OE Mail RIDSNRRDIRS PUBLIC RidsNrrPMTurkeyPoint Resource Enclosure U.S. NUCLEAR REGULATORY COMMISSION REGION II Docket Nos.: 50-250, 50-251 | |||
License Nos.: DPR-31, DPR-41 | |||
Report No: 05000250/2012005, 05000251/2012005 | |||
Licensee: Florida Power & Light Company (FPL) | |||
Facility: Turkey Point Nuclear Plant, Units 3 & 4 | |||
Location: 9760 S. W. 344th Street Homestead, FL 33035 | |||
Dates: October 1, 2012 to December 31, 2012 | |||
Inspectors: J. Stewart, Senior Resident Inspector T. Hoeg, Senior Resident Inspector P. Capehart, Senior Operations Engineer C. Fletcher, Senior Reactor Inpsector M. Barillas, Resident Inspector A. Vargas, Reactor Inspector M. Coursey, Reactor Inspector | |||
R. Taylor, Senior Project Engineer D. Mas-Penaranda, Project Engineer A. Zoulis, Senior Risk Analyst J. Laughlin, Emergency Preparedness Inspector G. Kuzo, Senior Health Physicist W. Pursley, Health Physicist Approved by: S. Sandal, Acting Chief Reactor Projects Branch 3 | |||
Division of Reactor Projects Enclosure | |||
=SUMMARY OF FINDINGS= | =SUMMARY OF FINDINGS= | ||
IR 05000250/2012005, 05000251/2012005; 10/01/2012 - 12/31/2012; Turkey Point Nuclear Power Plant, Units 3 and 4; Licensed Operator Requalification Program | IR 05000250/2012005, 05000251/2012005; 10/01/2012 - 12/31/2012; Turkey Point Nuclear Power Plant, Units 3 and 4; Licensed Operator Requalification Program | ||
The report covered a three month period of inspection by resident inspectors and region based inspectors. One Green Finding was identified. The significance of inspection findings are identified by their color i.e. (greater than Green, or Green, White, Yellow, or Red) and determined using Inspection Manual Chapter (IMC) 0609, "Significance Determination Process" (SDP) dated June 2, 2011. The cross-cutting aspect was determined using IMC 310, Components Within the Cross-Cutting Areas" dated October 28, 2011. All violations of NRC requirements are dispositioned in accordance with the NRC's Enforcement Policy dated June 7, 2012. The NRC's program for overseeing the safe operation of commercial nuclear power reactors is described in NUREG-1649, " | The report covered a three month period of inspection by resident inspectors and region based inspectors. One Green Finding was identified. The significance of inspection findings are identified by their color i.e. (greater than Green, or Green, White, Yellow, or Red) and determined using Inspection Manual Chapter (IMC) 0609, "Significance Determination Process" (SDP) dated June 2, 2011. The cross-cutting aspect was determined using IMC 310, Components Within the Cross-Cutting Areas" dated October 28, 2011. All violations of NRC requirements are dispositioned in accordance with the NRC's Enforcement Policy dated June 7, 2012. The NRC's program for overseeing the safe operation of commercial nuclear power reactors is described in NUREG-1649, "Reac tor Oversight Process," Revision 4. | ||
===Cornerstone: Initiating Events=== | ===Cornerstone: Initiating Events=== | ||
* Green: A self-revealing finding was identified when the licensee failed to follow procedure 0-ADM-222, Drain and Vent Rig Controls, while installing a temporary drain hose on Turkey Point Unit 4 in-service equipment. Operations and maintenance workers failed to verify a drain line flow path was isolated on the 1B feed water heater prior to removing a pipe valve cap that resulted in an unexpected lowering of condenser vacuum. Operators took action to close the open drain line isolation valve and terminate the plant transient. The licensee captured this condition in their corrective action program as AR 1819010. The licensee's failure to verify the closed position of 1B feed water heater drain valve 4-30-128, as required by procedure 0-ADM-222, prior to removing the pipe cap was a performance deficiency. The inspectors determined the performance deficiency was more than minor using IMC 0612, Appendix B, Issue Screening, because the performance deficiency was associated with the configuration control attribute of the initiating events cornerstone, and adversely affected the cornerstone objective to limit the likelihood of events that upset plant stability and challenge critical safety functions during power operations. Specifically, the failure to verify the position of 4-30-128 resulted in lowering condenser vacuum that could have led to a reactor trip and the unavailability of the main condenser. The inspectors evaluated the finding using the significance determination process for findings at power of IMC 0609, Appendix A, | * Green: A self-revealing finding was identified when the licensee failed to follow procedure 0-ADM-222, Drain and Vent Rig Controls, while installing a temporary drain hose on Turkey Point Unit 4 in-service equipment. Operations and maintenance workers failed to verify a drain line flow path was isolated on the 1B feed water heater prior to removing a pipe valve cap that resulted in an unexpected lowering of condenser vacuum. Operators took action to close the open drain line isolation valve and terminate the plant transient. The licensee captured this condition in their corrective action program as AR 1819010. | ||
The licensee's failure to verify the closed position of 1B feed water heater drain valve 4-30-128, as required by procedure 0-ADM-222, prior to removing the pipe cap was a performance deficiency. The inspectors determined the performance deficiency was more than minor using IMC 0612, Appendix B, Issue Screening, because the performance deficiency was associated with the configuration control attribute of the initiating events cornerstone, and adversely affected the cornerstone objective to limit the likelihood of events that upset plant stability and challenge critical safety functions during power operations. Specifically, the failure to verify the position of 4-30-128 resulted in lowering condenser vacuum that could have led to a reactor trip and the unavailability of the main condenser. The inspectors evaluated the finding using the significance determination process for findings at power of IMC 0609, Appendix A, | |||
Exhibit 1, Transient Initiators. The inspectors determined the finding was of very low safety significance (Green) because the finding did not result in a reactor trip and a loss of mitigation equipment relied upon to transition the plant to a stable shutdown condition. | Exhibit 1, Transient Initiators. The inspectors determined the finding was of very low safety significance (Green) because the finding did not result in a reactor trip and a loss of mitigation equipment relied upon to transition the plant to a stable shutdown condition. | ||
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=REPORT DETAILS= | =REPORT DETAILS= | ||
Summary of Plant Status: Unit 3 began the period at 29 percent power while adjustments were made to secondary plant chemistry. Unit 3 reached full power on November 16, 2012, where they remained through the remainder of this inspection period. | |||
===Summary of Plant Status=== | |||
: Unit 3 began the period at 29 percent power while adjustments were made to secondary plant chemistry. Unit 3 reached full power on November 16, 2012, where they remained through the remainder of this inspection period. | |||
Unit 4 began this inspection period at full power. On November 4, 2012, reactor power was reduced to 30 percent to support secondary plant testing. On November 5, 2012, the unit was shut down to begin a refueling and extended power uprate outage. | Unit 4 began this inspection period at full power. On November 4, 2012, reactor power was reduced to 30 percent to support secondary plant testing. On November 5, 2012, the unit was shut down to begin a refueling and extended power uprate outage. | ||
==REACTOR SAFETY== | ==REACTOR SAFETY== | ||
Cornerstones: Initiating Events, Mitigating Systems, Barrier Integrity | Cornerstones: Initiating Events, Mitigating Systems, Barrier Integrity | ||
{{a|1R04}} | |||
==1R04 Equipment Alignment== | |||
===.1 Partial Equipment Walkdowns=== | ===.1 Partial Equipment Walkdowns=== | ||
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====a. Inspection Scope==== | ====a. Inspection Scope==== | ||
Non-Destructive Examination Activities and Welding Activities: From November 13-16 and December 10-14, 2012, the inspectors conducted an on-site review of the implementation of the licensee's In-service Inspection (ISI) Program for monitoring degradation of the reactor coolant system, emergency feed water systems, risk-significant piping and components, and containment systems in Unit 4. The inspectors' activities included a review of non-destructive examinations (NDEs) to evaluate compliance with the applicable edition of the American Society of Mechanical Engineers (ASME) Boiler and Pressure Vessel Code (BPVC), Section XI (Code of record: 2001 Edition with 2003 Addenda, | Non-Destructive Examination Activities and Welding Activities | ||
: From November 13-16 and December 10-14 , 2012, the inspectors conducted an on-site review of the implementation of the licensee's In-service Inspection (ISI) Program for monitoring degradation of the reactor coolant system, emergency feed water systems, risk-significant piping and components, and containment systems in Unit 4. The inspectors' activities included a review of non-destructive examinations (NDEs) to evaluate compliance with the applicable edition of the American Society of Mechanical Engineers (ASME) Boiler and Pressure Vessel Code (BPVC), Section XI (Code of record: 2001 Edition with 2003 Addenda, 4 th Interval, 3 rd Period and 1 st Outage), and to verify that indications and defects (if present) were appropriately evaluated in accordance with the requirements of the ASME Code, Section XI, acceptance standards. | |||
The inspectors directly observed and reviewed records for the following NDE mandated by the ASME Code to evaluate compliance with the ASME Code Section XI and Section V requirements and, if any indications and defects were detected, to evaluate if they were dispositioned in accordance with the ASME Code or an NRC-approved alternative requirement. | The inspectors directly observed and reviewed records for the following NDE mandated by the ASME Code to evaluate compliance with the ASME Code Section XI and Section V requirements and, if any indications and defects were detected, to evaluate if they were dispositioned in accordance with the ASME Code or an NRC-approved alternative requirement. | ||
* Visual Testing (VT): o Residual Heat Removal (RHR) to Reactor Coolant System (RCS) Loop C Cold Leg Spring Loaded and Constant Weight Hanger, No. SR-499, o RHR to RCS Loop C Cold Leg Double Acting Restraint Hanger, No. 8073-H-810-02, and o Reactor Vessel Bottom Mounted Instrumentation Penetration No. 1, 10, 7, 6, 25, 29, 24, 27, 47, 32, 16 and 42. | * Visual Testing (VT): | ||
* Augmented VT: o Pressurizer Heater Sleeves, No. 4-PRZ-Heater Sleeves, o High Head Safety Injection (HHSI) Loop A Inside Containment Pipe to Branch Connection, Weld No. 2-SI-1404-10, o HHSI Loop A Inside Containment Pipe to Elbow Connection, Weld No. 2-SI-1404-6, o Chemical Volume Control System (CVCS) to RCS Loop C Hot Leg Elbow to Branch Connection, Weld No. 3-CH-1401-37, and o CVCS to RCS Loop C Hot Leg Pipe to Elbow Connection, Weld No. 3-CH-1401-34. | o Residual Heat Removal (RHR) to Reactor Coolant System (RCS) Loop C Cold Leg Spring Loaded and Constant Weight Hanger, No. SR-499, o RHR to RCS Loop C Cold Leg Double Acting Restraint Hanger, No. 8073-H-810-02, and o Reactor Vessel Bottom Mounted Instrumentation Penetration No. 1, 10, 7, 6, 25, 29, 24, 27, 47, 32, 16 and 42. | ||
* Ultrasonic Testing (UT): o RHR to RCS Loop C Cold Leg Elbow to Pipe Weld No. 10-SI-1403-4 | * Augmented VT: | ||
* Augmented UT: o HHSI Loop A Inside Containment Pipe to Branch Connection, Weld No. 2-SI-1404-10, o HHSI Loop A Inside Containment Pipe to Elbow Connection, Weld No. 2-SI-1404-6, o CVCS to RCS Loop C Hot Leg Elbow to Branch Connection, Weld No. 3-CH-1401-37, and o CVCS to RCS Loop C Hot Leg Pipe to Elbow Connection, Weld No. 3-CH-1401-34. | o Pressurizer Heater Sleeves, No. 4-PRZ-Heater Sleeves, o High Head Safety Injection (HHSI) Loop A Inside Containment Pipe to Branch Connection, Weld No. 2-SI-1404-10, o HHSI Loop A Inside Containment Pipe to Elbow Connection, Weld No. 2-SI-1404-6, o Chemical Volume Control System (CVCS) to RCS Loop C Hot Leg Elbow to Branch Connection, Weld No. 3-CH-1401-37, and o CVCS to RCS Loop C Hot Leg Pipe to Elbow Connection, Weld No. 3-CH-1401-34. | ||
* Penetrant Testing (PT): o HHSI Socket to Pipe, Weld No. 2-SI-2406-2 The inspectors reviewed the welding activities referenced below and reviewed associated documents in order to evaluate compliance with procedures and the ASME Code. The inspectors reviewed the following work order, repair and replacement plan, weld data sheets, welding procedures, procedure qualification records, welder performance qualification records, and NDE reports. | * Ultrasonic Testing (UT): | ||
o RHR to RCS Loop C Cold Leg Elbow to Pipe Weld No. 10-SI-1403-4 | |||
* Augmented UT: | |||
o HHSI Loop A Inside Containment Pipe to Branch Connection, Weld No. 2-SI-1404-10, o HHSI Loop A Inside Containment Pipe to Elbow Connection, Weld No. 2-SI-1404-6, o CVCS to RCS Loop C Hot Leg Elbow to Branch Connection, Weld No. 3-CH-1401-37, and o CVCS to RCS Loop C Hot Leg Pipe to Elbow Connection, Weld No. 3-CH-1401-34. | |||
* Penetrant Testing (PT): | |||
o HHSI Socket to Pipe, Weld No. 2-SI-2406-2 The inspectors reviewed the welding activities referenced below and reviewed associated documents in order to evaluate compliance with procedures and the ASME Code. The inspectors reviewed the following work order, repair and replacement plan, weld data sheets, welding procedures, procedure qualification records, welder performance qualification records, and NDE reports. | |||
* Work Order (WO) No. 40010356-01, Replace 2" line in Boric Acid Solenoid t CVCS Valve 4-368, Class 2, and | * Work Order (WO) No. 40010356-01, Replace 2" line in Boric Acid Solenoid t CVCS Valve 4-368, Class 2, and | ||
* WO 38015275-01, Instrument Air Valve 4-40-336A and Carbon Steel Piping Replacement with Carbon Steel, Class 2, and | * WO 38015275-01, Instrument Air Valve 4-40-336A and Carbon Steel Piping Replacement with Carbon Steel, Class 2, and | ||
* WO 40078181-01, Removal of HHSI Pipe weld defects, Class 2. | * WO 40078181-01, Removal of HHSI Pipe weld defects, Class 2. | ||
During non-destructive surface and | During non-destructive surface and volum etric examinations performed since the previous refuelling outage, the licensee did not identify any relevant indications that were analytically evaluated and accepted for continued service. Therefore, no NRC review was completed for this inspection procedure attribute. | ||
PWR Vessel Upper Head Penetration (VUHP) Inspection Activities: For the Unit 4 vessel head, a bare metal visual examination was required this outage pursuant to 10 CFR 50.55a. The inspectors observed portions of the Unit 4 bare metal visual examination and reviewed NDE reports for VUHPs Nos. 7, 19, 28, 33, and 41 to determine if the activities, including the disposition of indications and defects, were conducted in accordance with the requirements of ASME Code Case N-729-1 and 10 CFR 50.55a(g)(6)(ii)(D). In particular, the inspectors evaluated if the required visual examination scope/coverage was achieved and limitations (if applicable) were recorded in accordance with the licensee procedures. Additionally, the inspectors evaluated if the licensee's criteria for visual examination quality and instructions for resolving interference and masking issues were consistent with 10 CFR 50.55a. | |||
The licensee did not identify any relevant indications that were accepted for continued service during the Unit 4 bare metal visual exams. Additionally, the licensee did not perform any welding repairs to the vessel head penetrations since the beginning of the last Unit 4 refueling outage. Therefore, no NRC review was completed for the refueling outage. Therefore, no NRC review was completed for these inspection procedure attributes. | The licensee did not identify any relevant indications that were accepted for continued service during the Unit 4 bare metal visual exams. Additionally, the licensee did not perform any welding repairs to the vessel head penetrations since the beginning of the last Unit 4 refueling outage. Therefore, no NRC review was completed for the refueling outage. Therefore, no NRC review was completed for these inspection procedure attributes. | ||
Boric Acid Corrosion Control (BACC) Inspection Activities: The inspectors reviewed the licensee's BACC program activities to ensure implementation with commitments made in response to NRC Generic Letter 88-05, "Boric Acid Corrosion of Carbon Steel Reactor Pressure Boundary," and applicable industry guidance documents. Specifically, the inspectors performed an on-site record review of procedures and the results of the licensee's containment walk-down inspections performed during the current fall refueling outage. The inspectors also interviewed the BACC program owner, conducted an independent walk-down of containment to evaluate compliance with licensee's BACC program requirements, and verified that degraded or non-conforming conditions, such as boric acid leaks, were properly identified and corrected in accordance with the licensee's BACC and corrective action programs. The inspectors reviewed the following engineering evaluations completed for evidence of boric acid identified in systems containing borated water to determine if degraded components were documented in the corrective action program. The inspectors also evaluated the following corrective actions for any degraded components to determine if they met the ASME Section XI Code and/or NRC approved alternative. | Boric Acid Corrosion Control (BACC) Inspection Activities: The inspectors reviewed the licensee's BACC program activities to ensure implementation with commitments made in response to NRC Generic Letter 88-05, "Boric Acid Corrosion of Carbon Steel Reactor Pressure Boundary," and applicable industry guidance documents. Specifically, the inspectors performed an on-site record review of procedures and the results of the licensee's containment walk-down inspections performed during the current fall refueling outage. The inspectors also interviewed the BACC program owner, conducted an independent walk-down of containment to evaluate compliance with licensee's BACC program requirements, and verified that degraded or non-conforming conditions, such as boric acid leaks, were properly identified and corrected in accordance with the licensee's BACC and corrective action programs. | ||
The inspectors reviewed the following engineering evaluations completed for evidence of boric acid identified in systems containing borated water to determine if degraded | |||
components were documented in the corrective action program. The inspectors also evaluated the following corrective actions for any degraded components to determine if they met the ASME Section XI Code and/or NRC approved alternative. | |||
* AR 01685161 | * AR 01685161 | ||
* AR 01703036 | * AR 01703036 | ||
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* Reviewed ET personnel qualifications. | * Reviewed ET personnel qualifications. | ||
Identification and Resolution of Problems: The inspectors performed a review of a sample of ISI-related problems which were identified by the licensee and entered into the corrective action program as condition reports (ARs). The inspectors reviewed the ARs to confirm the licensee had appropriately described the scope of the problem, and had initiated corrective actions. The review also included the licensee's consideration and assessment of operating experience events applicable to the plant. The inspectors performed this review to ensure compliance with 10CFR Part 50, Appendix B, Criterion XVI, "Corrective Action," requirements. Document reviewed are listed in the Attachment. | Identification and Resolution of Problems: The inspectors performed a review of a sample of ISI-related problems which were identified by the licensee and entered into the corrective action program as condition reports (ARs). The inspectors reviewed the ARs to confirm the licensee had appropriately described the scope of the problem, and had initiated corrective actions. The review also included the licensee's consideration and assessment of operating experience events applicable to the plant. The inspectors | ||
performed this review to ensure compliance with 10CFR Part 50, Appendix B, Criterion XVI, "Corrective Action," requirements. Document reviewed are listed in the Attachment. | |||
====b. Findings==== | ====b. Findings==== | ||
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* Use of human error prevention techniques such as peer checks | * Use of human error prevention techniques such as peer checks | ||
* Documentation of activities, including initials and sign-offs in procedures | * Documentation of activities, including initials and sign-offs in procedures | ||
* Supervision of activities, including risk and reactivity management oversight | * Supervision of activities, including risk and reactivity management oversight This activity constituted four inspection samples. | ||
====b. Findings==== | ====b. Findings==== | ||
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On November 1, 2012, Turkey Point Nuclear Plant Unit 4 experienced an unexpected lowering of condenser vacuum due to the removal of a drain valve pipe cap on the 1B feed water heater. The non-safety related upstream drain isolation valve (4-30-128) was not physically verified to be in its normal closed position as required by safety-related procedure 0-ADM-222, Drain and Vent Rig Controls, prior to removing the pipe cap. | On November 1, 2012, Turkey Point Nuclear Plant Unit 4 experienced an unexpected lowering of condenser vacuum due to the removal of a drain valve pipe cap on the 1B feed water heater. The non-safety related upstream drain isolation valve (4-30-128) was not physically verified to be in its normal closed position as required by safety-related procedure 0-ADM-222, Drain and Vent Rig Controls, prior to removing the pipe cap. | ||
The licensee used procedure 0-ADM-222 as governing guidance to perform both safety and non-safety related plant operations. Unit 4 was in Mode 1, at 100 percent power when the operator at the controls noticed a drop from 762 to 714 megawatts electric (MWe) and a lowering of | The licensee used procedure 0-ADM-222 as governing guidance to perform both safety and non-safety related plant operations. Unit 4 was in Mode 1, at 100 percent power when the operator at the controls noticed a drop from 762 to 714 megawatts electric (MWe) and a lowering of con denser vacuum from 27.7" mercury (Hg) to 26.0" Hg. The operations work control department had authorized mechanical maintenance to install a drain hose on the in-service 1B feed water heater shell in preparation for the upcoming refueling outage. Instead of physically verifying the position of valve 4-30-128 as required by procedure 0-ADM-222, the licensee relied on their work clearance control computer tracking system to check the position of the valve and incorrectly concluded that the drain valve was closed. As a result, an air in-leakage path was created by mechanical maintenance when the pipe cap downstream of the valve was removed to connect the drain hos e. Off normal operating procedure 4-ONOP-014, Main Condenser Loss of Vacuum, was entered when operators at the controls noticed an unexpected lowering in condenser vacuum. The mechanical maintenance workers immediately notified Operations department they had just installed a drain rig assembly on the feed water heater shell drain valve and coordinated with the operators to close the drain valve which restored vacuum and the plant transient was terminated. The licensee entered this issue into their corrective action program as AR 1819010. | ||
=====Analysis:===== | =====Analysis:===== | ||
The licensee's failure to verify the closed position of 1B feed water heater drain valve 4-30-128, as required by | The licensee's failure to verify the closed position of 1B feed water heater drain valve 4-30-128, as required by procedur e 0-ADM-222, prior to removing the pipe cap was a performance deficiency. The inspectors determined the performance deficiency was more than minor using IMC 0612, Appendix B, Issue Screening, because the performance deficiency was associated with the configuration control attribute of the initiating events cornerstone, and adversely affected the cornerstone objective to limit the likelihood of events that upset plant stability and challenge critical safety functions during power operations. Specifically, the failure to verify the position of 4-30-128 resulted in lowering condenser vacuum that could have led to a reactor trip and the unavailability of the main condenser. The inspectors evaluated the finding using the significance determination process for findings at power of IMC 0609, Appendix A, Exhibit 1, Transient Initiators. The inspectors determined the finding was of very low safety significance (Green) because the finding did not result in a reactor trip and a loss of mitigation equipment relied upon to transition the plant to a stable shutdown condition. | ||
The finding was associated with a cross-cutting aspect in the work practices component of the human performance area because the licensee did not define and effectively communicate expectations, or follow the procedural requirement to physically verify valve position during the drain hose installation work. [H.4(b) per IMC 0310] | The finding was associated with a cross-cutting aspect in the work practices component of the human performance area because the licensee did not define and effectively communicate expectations, or follow the procedural requirement to physically verify valve position during the drain hose installation work. [H.4(b) per IMC 0310] | ||
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====a. Inspection Scope==== | ====a. Inspection Scope==== | ||
The inspectors completed in-office reviews and control room inspections of the licensee's risk assessment of four emergent or planned maintenance activities. The inspectors verified the licensee's risk assessment and risk management activities using the requirements of 10 CFR 50.65(a)(4); the recommendations of Nuclear Management and Resource Council 93-01, Industry Guidelines for Monitoring the Effectiveness of Maintenance at Nuclear Power Plants, Revision 3; and procedures 0-ADM-068, Work Week Management; WM-AA-1000, Work Activity Risk Management; and O-ADM-225, On Line Risk Assessment and Management. The inspectors also reviewed the effectiveness of the licensee's contingency actions to mitigate increased risk resulting from the degraded equipment and the licensee assessment of aggregate risk using FPL procedure OP-AA-104-1007, Online Aggregate Risk. The inspectors evaluated the following risk assessments during the inspection: | The inspectors completed in-office reviews and control room inspections of the licensee's risk assessment of four emergent or planned maintenance activities. The inspectors verified the licensee's risk assessment and risk management activities using the requirements of 10 CFR 50.65(a)(4); the recommendations of Nuclear Management and Resource Council 93-01, Industry Guidelines for Monitoring the Effectiveness of Maintenance at Nuclear Power Plants, Revision 3; and procedures 0-ADM-068, Work Week Management; WM-AA-1000, Work Activity Risk Management; and O-ADM-225, On Line Risk Assessment and Management. The inspectors also reviewed the effectiveness of the licensee's contingency actions to mitigate increased risk resulting from the degraded equipment and the licensee assessment of aggregate risk using FPL procedure OP-AA-104-1007, Online Aggregate Risk. The inspectors evaluated the following risk assessments during the inspection: | ||
* October 25: Unit 3 risk assessment when auxiliary feed water train 2 flow control valves FCV-3-2831 and FCV-3-2832 were removed from service for maintenance, B standby steam generator feed water pump | * October 25: Unit 3 risk assessment when auxiliary feed water train 2 flow control valves FCV-3-2831 and FCV-3-2832 were removed from service for maintenance, B standby steam generator feed water pump wa s out of service for maintenance, and severe weather threatened the region (Tropical Storm Sandy). The licensee's Green risk characterization was verified using NRC's Standardized Plant Analysis Risk (SPAR) Model for Turkey Point Unit 3 and 4 and risk assessment tool. | ||
* December 5: The performance of the Unit 3 risk assessment was verified and reviewed for accuracy using the licensee risk assessment tool during RCS Flow protection channel tests which requires associated bistables to be tripped. The risk assessment evaluated the aggregate risk. The inspector's observed the use of the tool in the Work Control Center and the Control Room and reviewed the Equipment Out of Service book and Operator Logs to verify the plant configuration. The licensee's Green risk characterization was verified using the NRC's SPAR Model for Turkey Point Unit 3 and 4 and risk assessment tool. | * December 5: The performance of the Unit 3 risk assessment was verified and reviewed for accuracy using the licensee risk assessment tool during RCS Flow protection channel tests which requires associated bistables to be tripped. The risk assessment evaluated the aggregate risk. The inspector's observed the use of the tool in the Work Control Center and the Control Room and reviewed the Equipment Out of Service book and Operator Logs to verify the plant configuration. The licensee's Green risk characterization was verified using the NRC's SPAR Model for Turkey Point Unit 3 and 4 and risk assessment tool. | ||
* December 11: Unit 3 risk assessment when 3A ICW/CCW Basket Strainer BS-3-1402 was removed from service for maintenance in conjunction with 4A 4kV bus, 4A emergency diesel generator, and the 4A high head safety injection pump. The licensee's Yellow risk | * December 11: Unit 3 risk assessment when 3A ICW/CCW Basket Strainer BS-3-1402 was removed from service for maintenance in conjunction with 4A 4kV bus, 4A emergency diesel generator, and the 4A high head safety injection pump. The licensee's Yellow risk characterizati on was verified using NRC's Standardized Plant Analysis Risk (SPAR) Model for Turkey Point Unit 3 and 4 and risk assessment tool. | ||
* December 13: Unit 3 risk management when the 3A emergency diesel generator fuel oil transfer pump failed to start during its quarterly surveillance test (AR 1832175) | * December 13: Unit 3 risk management when the 3A emergency diesel generator fuel oil transfer pump failed to start during its quarterly surveillance test (AR 1832175) | ||
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Modifications associated with the extended powerup rate (EPU) are noted. | Modifications associated with the extended powerup rate (EPU) are noted. | ||
* Unit 3: 3-OSP-203.2, Train B Engineered Safeguards Integrated Test, sections 7.2 and 7.3 in accordance with engineering change 273225, Emergency Containment Cooler (ECC) Auto-Start Circuit Installation, verifying auto start capability for the swing emergency containment cooler to mitigate a single active failure component and have two ECC units running (EPU) | * Unit 3: 3-OSP-203.2, Train B Engineered Safeguards Integrated Test, sections 7.2 and 7.3 in accordance with engineering change 273225, Emergency Containment Cooler (ECC) Auto-Start Circuit Installation, verifying auto start capability for the swing emergency containment cooler to mitigate a single active failure component | ||
and have two ECC units running (EPU) | |||
* Unit 3: RPS relay replacement and post maintenance testing in accordance with WO 40120591-01 and 3-OSP-049.1, Reactor Protection System Logic Test, after replacement of reactor coolant flow loop B relay RC-4-B, when it was found failed in its de-energized state. | * Unit 3: RPS relay replacement and post maintenance testing in accordance with WO 40120591-01 and 3-OSP-049.1, Reactor Protection System Logic Test, after replacement of reactor coolant flow loop B relay RC-4-B, when it was found failed in its de-energized state. | ||
* Unit 3: 3A Train PRB-1-A, power range block permissive relay found de-energized per WO 40195473-01. The post maintenance test was performed in accordance with procedures contained in the referenced work order and 3-OSP-049.1, Reactor Protection System Logic Test, after replacement of the power range block permissive relay PRB-1-A. | * Unit 3: 3A Train PRB-1-A, power range block permissive relay found de-energized per WO 40195473-01. The post maintenance test was performed in accordance with procedures contained in the referenced work order and 3-OSP-049.1, Reactor Protection System Logic Test, after replacement of the power range block permissive relay PRB-1-A. | ||
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====a. Inspection Scope==== | ====a. Inspection Scope==== | ||
The inspectors either reviewed or witnessed the six surveillance tests listed below to verify that the tests met the TS requirements, the UFSAR, and the licensee's procedural requirements and demonstrated that the | The inspectors either reviewed or witnessed the six surveillance tests listed below to verify that the tests met the TS requirements, the UFSAR, and the licensee's procedural requirements and demonstrated that the syst ems were operationally ready to perform their intended safety functions. In addition, the inspectors evaluated the effect of the testing activities on the plant to ensure that conditions were adequately addressed by the licensee staff and that after completion of the testing activities, equipment was returned to the alignment required for the system to perform its safety function. In-service tests (IST) were validated using the licensee's In-service Testing Program, Fourth Ten Year Interval, dated March 11, 2004. The inspectors verified that surveillance issues were documented in the corrective action program. Extended power uprate (EPU) testing was done under NRC Inspection Procedure 71004 guidance. | ||
Containment Isolation Valve Test: | Containment Isolation Valve Test | ||
* 3-OSP-206.2, Quarterly In-service Valve Testing - Containment Isolation Valve | : | ||
* 3-OSP-206.2, Quarterly In-service Valve Testing - Containment Isolation Valve Surveillance Test | |||
: | |||
* 0-OSP-207.2, Visual Leak Inspection of Systems Outside Containment, Section 7.6.4 Visual Inspection of Unit 4 Volume Control Tank Room | * 0-OSP-207.2, Visual Leak Inspection of Systems Outside Containment, Section 7.6.4 Visual Inspection of Unit 4 Volume Control Tank Room | ||
* 0-OSP-005.3, Load Testing of the Station Blackout Cross-Tie | * 0-OSP-005.3, Load Testing of the Station Blackout Cross-Tie | ||
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===Cornerstone:=== | ===Cornerstone:=== | ||
Emergency Preparedness | Emergency Preparedness 1EP4 Emergency Action Level and Emergency Plan Changes | ||
====a. Inspection Scope==== | ====a. Inspection Scope==== | ||
The Nuclear Security and Incident Response (NSIR) headquarters staff performed an in-office review of the latest revisions of various Emergency Plan Implementing Procedures (EPIPs) and the Emergency Plan located under ADAMS accession numbers ML12009A082 and ML12184A052, as listed in the Attachment. The licensee determined that in accordance with 10 CFR 50.54(q), the changes made in the revisions resulted in no reduction in the effectiveness of the Plan, and that the revised Plan continued to meet the requirements of 10 CFR 50.47(b) and Appendix E to 10 CFR Part 50. The NRC review was not documented in a safety evaluation report and did not constitute approval of licensee-generated changes; therefore, these revisions are subject to future inspection. Documents reviewed are listed in the Attachment. This inspection activity satisfied one inspection sample for the emergency action level and emergency plan changes on an annual basis. | The Nuclear Security and Incident Response (NSIR) headquarters staff performed an in-office review of the latest revisions of various Emergency Plan Implementing Procedures (EPIPs) and the Emergency Plan located under ADAMS accession numbers ML12009A082 and ML12184A052, as listed in the Attachment. | ||
The licensee determined that in accordance with 10 CFR 50.54(q), the changes made in the revisions resulted in no reduction in the effectiveness of the Plan, and that the revised Plan continued to meet the requirements of 10 CFR 50.47(b) and Appendix E to 10 CFR Part 50. The NRC review was not documented in a safety evaluation report and did not constitute approval of licensee-generated changes; therefore, these revisions are subject to future inspection. Documents reviewed are listed in the Attachment. This inspection activity satisfied one inspection sample for the emergency action level and emergency plan changes on an annual basis. | |||
====b. Findings==== | ====b. Findings==== | ||
No findings were identified. 1EP6 Drill Evaluation | No findings were identified. | ||
1EP6 Drill Evaluation | |||
===.1 Emergency Preparedness Drill=== | ===.1 Emergency Preparedness Drill=== | ||
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==RADIATION SAFETY== | ==RADIATION SAFETY== | ||
Cornerstones: Occupational Radiation Safety (OS) and Public Radiation Safety (PS) | Cornerstones: Occupational Radiation Safety (OS) and Public Radiation Safety (PS) | ||
{{a|2RS1}} | {{a|2RS1}} | ||
==2RS1 Radiological Hazard Assessment and Exposure Controls== | ==2RS1 Radiological Hazard Assessment and Exposure Controls== | ||
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Contamination and Radioactive Material Control: The inspectors observed surveys of material and personnel being released from the RCA using small article monitor (SAM), personnel contamination monitor, and portal monitor instrumentation. SAM equipment sensitivity, alarm set-points, and release program guidance were discussed with licensee staff. The inspectors also reviewed records of leak tests on selected sealed sources, discussed nationally tracked source transactions with licensee staff, and verified sources within select storage locations. The inspectors also reviewed and discussed with staff processes for release of turbine building components and materials being replaced as part of the ongoing extended power up-rate activities. | Contamination and Radioactive Material Control: The inspectors observed surveys of material and personnel being released from the RCA using small article monitor (SAM), personnel contamination monitor, and portal monitor instrumentation. SAM equipment sensitivity, alarm set-points, and release program guidance were discussed with licensee staff. The inspectors also reviewed records of leak tests on selected sealed sources, discussed nationally tracked source transactions with licensee staff, and verified sources within select storage locations. The inspectors also reviewed and discussed with staff processes for release of turbine building components and materials being replaced as part of the ongoing extended power up-rate activities. | ||
Radiological Hazards Control and Work Coverage: Licensee controls for areas where dose rates could change significantly as a result of plant shutdown and refueling operations were reviewed and discussed. The inspectors reviewed RWPs for work within airborne radioactivity areas. For potential HRA tasks involving significant dose rate gradients, e.g., bottom mounted instrumentation maintenance conducted within the reactor sump, the inspectors evaluated the use and placement of whole body and extremity dosimetry to monitor worker exposure. Controls and their implementation for storage of irradiated material within the U4 spent fuel pool (SFP) were reviewed and discussed with responsible licensee representatives. | Radiological Hazards Control and Work Coverage: Licensee controls for areas where dose rates could change significantly as a result of plant shutdown and refueling operations were reviewed and discussed. The inspectors reviewed RWPs for work within airborne radioactivity areas. For potential HRA tasks involving significant dose rate gradients, e.g., bottom mounted instrumentation maintenance conducted within the reactor sump, the inspectors evaluated the use and placement of whole body and | ||
extremity dosimetry to monitor worker exposure. Controls and their implementation for storage of irradiated material within the U4 spent fuel pool (SFP) were reviewed and discussed with responsible licensee representatives. | |||
Risk-Significant High Radiation Area and Very High Radiation Area Controls: The inspectors evaluated access barrier effectiveness of Locked High Radiation Area (LHRA) and Very High Radiation Area (VHRA) controls for selected U4 containment building and U3 and 4 reactor auxiliary building (RAB) locations. Procedures for LHRA and VHRA controls were discussed with health physics (HP) supervisors. | Risk-Significant High Radiation Area and Very High Radiation Area Controls | ||
: The inspectors evaluated access barrier effectiveness of Locked High Radiation Area (LHRA) and Very High Radiation Area (VHRA) controls for selected U4 containment building and U3 and 4 reactor auxiliary building (RAB) locations. Procedures for LHRA and VHRA controls were discussed with health physics (HP) supervisors. | |||
Radiation Worker Performance and Radiation Protection Technician Proficiency: Occupational worker adherence to selected RWPs and Radiation Protection Technician (RPT) proficiency in providing U4 containment and RAB job coverage were evaluated through direct observations and discussions with licensee staff. | Radiation Worker Performance and Radiation Protection Technician Proficiency | ||
: Occupational worker adherence to selected RWPs and Radiation Protection Technician (RPT) proficiency in providing U4 containment and RAB job coverage were evaluated through direct observations and discussions with licensee staff. | |||
Problem Identification and Resolution: Corrective Action Program (CAP) documents associated with radiological hazard assessment and control were reviewed and assessed. The inspectors evaluated the licensee's ability to identify and resolve the issues in accordance with Performance Improvement procedure (PI)-AA-01, Corrective Action Program and Condition Reporting, Revision (Rev.) 3 and PI-AA-204, Condition Identification and Screening Process, Rev. 18. The inspectors also evaluated the scope of the licensee's internal audit program and reviewed recent assessment results. | Problem Identification and Resolution: Corrective Action Program (CAP) documents associated with radiological hazard assessment and control were reviewed and assessed. The inspectors evaluated the licensee's ability to identify and resolve the issues in accordance with Performance Improvement procedure (PI)-AA-01, Corrective Action Program and Condition Reporting, Revision (Rev.) 3 and PI-AA-204, Condition Identification and Screening Process, Rev. 18. The inspectors also evaluated the scope of the licensee's internal audit program and reviewed recent assessment results. | ||
Radiation protection activities were evaluated against the requirements of Updated Final Safety Analysis Report (UFSAR) Section 11; Technical Specifications (TS) Sections 6.8 Procedures and Programs and 6.12 HRA; 10 CFR Parts 19 and 20; and approved licensee procedures. Licensee programs for monitoring materials and personnel released from the RCA were evaluated against 10 CFR Part 20 and IE Circular 81-07, Control of Radioactively Contaminated Material. Documents reviewed are listed in the | Radiation protection activities were evaluated against the requirements of Updated Final Safety Analysis Report (UFSAR) Section 11; Technical Specifications (TS) Sections 6.8 Procedures and Programs and 6.12 HRA; 10 CFR Parts 19 and 20; and approved licensee procedures. Licensee programs for monitoring materials and personnel released from the RCA were evaluated against 10 CFR Part 20 and IE Circular 81-07, Control of Radioactively Contaminated Material. Documents reviewed are listed in the | ||
. | |||
The inspectors completed one sample as required by inspection procedure 71124.01. | The inspectors completed one sample as required by inspection procedure 71124.01. | ||
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For dry active waste (DAW) generated during recent Unit 3 reactor sump and RWST maintenance activities, the inspectors evaluated analyses for hard-to-detect nuclides, reviewed the use of scaling factors, and discussed quality assurance (QA) activities for the waste stream characterizations by the current vendor analysis laboratory. The waste stream sampling methodologies and the resultant data used in select shipping and waste processing activities were evaluated and discussed with responsible radwaste staff. | For dry active waste (DAW) generated during recent Unit 3 reactor sump and RWST maintenance activities, the inspectors evaluated analyses for hard-to-detect nuclides, reviewed the use of scaling factors, and discussed quality assurance (QA) activities for the waste stream characterizations by the current vendor analysis laboratory. The waste stream sampling methodologies and the resultant data used in select shipping and waste processing activities were evaluated and discussed with responsible radwaste staff. | ||
Radioactive Material Storage: During walk-downs of radioactive material and radioactive waste storage areas, the inspectors observed the physical condition and labeling of storage containers and the posting of Radioactive Material Areas. The inspectors also reviewed licensee procedural guidance for storage and monitoring of radioactive material. Radiologically Controlled Area (RCA) storage areas evaluated included select Unit 3 and Unit 4 auxiliary building locations, Dry Storage Warehouse, main RCA yard material and waste storage areas, ISFSI facility, and the Radio Tower Road EPU Material Processing area. | Radioactive Material Storage | ||
: During walk-downs of radioactive material and radioactive waste storage areas, the inspectors observed the physical condition and labeling of storage containers and the posting of Radioactive Material Areas. The inspectors also reviewed licensee procedural guidance for storage and monitoring of radioactive material. Radiologically Controlled Area (RCA) storage areas evaluated included select Unit 3 and Unit 4 auxiliary building locations, Dry Storage Warehouse, main RCA yard material and waste storage areas, ISFSI facility, and the Radio Tower Road EPU Material Processing area. | |||
Radioactive Waste System Area Walkdowns: During inspector walk-downs, accessible sections of the liquid and solid radioactive waste (radwaste) processing systems were assessed for material condition and conformance with system design diagrams. | Radioactive Waste System Area Walkdowns | ||
: During inspector walk-downs, accessible sections of the liquid and solid radioactive waste (radwaste) processing systems were assessed for material condition and conformance with system design diagrams. | |||
Inspected equipment included radwaste processing and holdup tanks; radwaste system transfer piping, resin and filter components; dewatering system equipment and liquid radioactive waste control panel equipment. In addition, the inspectors reviewed the completion status of selected work order packages associated with liquid waste processing equipment | Inspected equipment included radwaste processing and holdup tanks; radwaste system transfer piping, resin and filter components; dewatering system equipment and liquid radioactive waste control panel equipment. In addition, the inspectors reviewed the completion status of selected work order packages associated with liquid waste processing equipment. | ||
Additional shipping records were reviewed for consistency with licensee procedures and compliance with NRC and DOT regulations. The inspectors reviewed emergency response information, DOT shipping package classification, and waste classification, radiation survey results. Licensee procedures for labeling containers stored onsite were evaluated. In addition, training status for selected individuals currently involved in radioactive material shipping activities was reviewed. Problem Identification and Resolution: The inspectors reviewed selected Corrective Action Program (CAP) documentation in the areas of radwaste processing and radwaste /radioactive material shipping. The inspectors evaluated the licensee's ability to identify and resolve identified issues in accordance with Performance Improvement procedure (PI)-AA-01, Corrective Action Program and Condition Reporting, Rev. 3, and PI-AA-204, Condition Identification and Screening Process, Rev 18. The inspectors also evaluated the scope of the licensee's internal audit program. | Transportation: During the onsite inspection, the inspectors directly observed and evaluated proficiency of the responsible staff during preparation of waste and material shipments. Training provided to radioactive waste staff responsible for preparation of | ||
the shipments to meet Department of Transportation (DOT) regulations was evaluated. | |||
Additional shipping records were reviewed for consistency with licensee procedures and compliance with NRC and DOT regulations. The inspectors reviewed emergency response information, DOT shipping package classification, and waste classification, radiation survey results. Licensee procedures for labeling containers stored onsite were evaluated. In addition, training status for selected individuals currently involved in radioactive material shipping activities was reviewed. | |||
Problem Identification and Resolution: The inspectors reviewed selected Corrective Action Program (CAP) documentation in the areas of radwaste processing and radwaste /radioactive material shipping. The inspectors evaluated the licensee's ability to identify and resolve identified issues in accordance with Performance Improvement procedure (PI)-AA-01, Corrective Action Program and Condition Reporting, Rev. 3, and PI-AA-204, Condition Identification and Screening Process, Rev 18. The inspectors also evaluated the scope of the licensee's internal audit program. | |||
Radwaste processing activities and equipment configuration were reviewed for compliance with the licensee's Process Control Program (PCP), UFSAR Chapter 11; TS 6.8.1, Procedures and Programs, and approved procedures. Waste stream characterization analyses were reviewed against regulations detailed in 10 CFR Part 20, 10 CFR Part 61, and guidance provided in the Branch Technical Position on Waste Classification (1983). Transportation program implementation was reviewed against regulations detailed in 10 CFR Part 20, 10 CFR Part 71, and 49 CFR Parts 172-178. | Radwaste processing activities and equipment configuration were reviewed for compliance with the licensee's Process Control Program (PCP), UFSAR Chapter 11; TS 6.8.1, Procedures and Programs, and approved procedures. Waste stream characterization analyses were reviewed against regulations detailed in 10 CFR Part 20, 10 CFR Part 61, and guidance provided in the Branch Technical Position on Waste Classification (1983). Transportation program implementation was reviewed against regulations detailed in 10 CFR Part 20, 10 CFR Part 71, and 49 CFR Parts 172-178. | ||
Training activities were assessed against 49 CFR Part 172 Subpart H. Documents reviewed are listed in the Attachment The inspectors completed one sample as required by inspection procedure 71124.08. | Training activities were assessed against 49 CFR Part 172 Subpart H. Documents reviewed are listed in the Attachment | ||
The inspectors completed one sample as required by inspection procedure 71124.08. | |||
====b. Findings==== | ====b. Findings==== | ||
No findings were identified | No findings were identified | ||
==OTHER ACTIVITIES== | ==OTHER ACTIVITIES== | ||
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====b. Findings==== | ====b. Findings==== | ||
No findings were identified. The inspectors did not identify any trends not observed by the licensee's trending activities. | No findings were identified. The inspectors did not identify any trends not observed by the licensee's trending activities. | ||
{{a|4OA3}} | {{a|4OA3}} | ||
==4OA3 Event Follow-up== | ==4OA3 Event Follow-up== | ||
===.1 (Closed) Licensee Event Report ( | ===.1 (Closed) Licensee Event Report (L=== | ||
While performing the Unit 3 Main Turbine Valve Alignment in preparation for turbine startup prior to entering Mode 1, operators discovered the turbine pressure transmitters PT-3-446 and PT-3-447 inadvertently isolated. The operator immediately notified the control room and the licensee entered Technical Specifications action statement 3.0.3 because two instrument channels were inoperable. The root isolation valves to the pressure transmitters were found closed and the operators subsequently opened the valves exiting the action statement. It | |||
ER) 50-250/2012-003-00 Condition Prohibited by Technical Specifications Due to Instrument Valve Mispositioning While performing the Unit 3 Main Turbine Valve Alignment in preparation for turbine startup prior to entering Mode 1, operators discovered the turbine pressure transmitters PT-3-446 and PT-3-447 inadvertently isolated. The operator immediately notified the control room and the licensee entered Technical Specifications action statement 3.0.3 because two instrument channels were inoperable. The root isolation valves to the pressure transmitters were found closed and the operators subsequently opened the valves exiting the action statement. It wa s determined that the valves were newly installed and mispositioned during the performance of an Engineering Modification. The root cause analysis documented in AR 1791236 identified a weakness in the Change Request Notice process that failed to identify plant procedure 3-NOP-089, Main Turbine, as an effected document. The licensee took additional actions to correct and prevent this from occurring in the future. The inspector did not identify any performance deficiency and determined that the technical specification non-compliance was of minor significance since it was self-revealing and did not have the potential to lead to a more significant safety concern. The LER is closed. | |||
===.2 (Closed) Licensee Event Report (LER) 50-250/2012-004-00 Condition Prohibited by Technical Specifications Due to Instrument Process Line Reversal During Replacement=== | ===.2 (Closed) Licensee Event Report (LER) 50-250/2012-004-00 Condition Prohibited by Technical Specifications Due to Instrument Process Line Reversal During Replacement=== | ||
After increasing power on Unit 3 and entering Mode 1, operators discovered the flow transmitter 3-FT-476, Channel IV Steam Generator 3A Main Feedwater Flow, was reading lower than expected compared to the other channels. The operator wrote an AR and a work request was issued to troubleshoot the issue. After further evaluation, the channel was declared inoperable and the unit entered Technical Specifications Limiting Condition of Operation 3.3.1,Table 3.3-1, Functional Unit 12 Action 6 which allows continued operation provided the inoperable channel is placed in the tripped condition within 6 hours. An investigation by maintenance personnel discovered the high and low sides of the process tubing for the transmitter 3-FT-476 were reversed. The process tubing was repaired and the site exited the action statement and restored the instrument channel. The process tubing for 3-FT-476 was reversed during the recent refueling outage work completed on May 19, 2012. The root cause analysis documented in AR 1800833 identified a weakness in the work instruction and inadequate post maintenance testing. The inspectors documented a self-revealing, non-cited violation (NCV 50-250,251/2012-004-01) of Turkey Point Technical Specification (TS) 3.3.1 Reactor Trip System Instrumentation in Inspection Report 05000250/2012004 and 05000251/20120004. No new findings were identified in the inspector's review of the LER and root cause analysis. The LER is closed. | |||
After increasing power on Unit 3 and entering Mode 1, operators discovered the flow | |||
transmitter 3-FT-476, Channel IV Steam Generator 3A Main Feedwater Flow, was reading lower than expected compared to the other channels. The operator wrote an AR and a work request was issued to troubleshoot the issue. After further evaluation, the channel was declared inoperable and the unit entered Technical Specifications Limiting Condition of Operation 3.3.1,Table 3.3-1, Functional Unit 12 Action 6 which allows continued operation provided the inoperable channel is placed in the tripped condition within 6 hours. An investigation by maintenance personnel discovered the high and low sides of the process tubing for the transmitter 3-FT-476 were reversed. The process tubing was repaired and the site exited the action statement and restored the instrument channel. The process tubing for 3-FT-476 was reversed during the recent refueling outage work completed on May 19, 2012. The root cause analysis documented in AR 1800833 identified a weakness in the work instruction and inadequate post maintenance testing. The inspectors documented a self-revealing, non-cited violation (NCV 50-250,251/2012-004-01) of Turkey Point Technical Specification (TS) 3.3.1 Reactor Trip System Instrumentation in Inspection Report 05000250/2012004 and 05000251/20120004. No new findings were identified in the inspector's review of the LER and root cause analysis. The LER is closed. | |||
{{a|4OA5}} | {{a|4OA5}} | ||
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====a. Inspection Scope==== | ====a. Inspection Scope==== | ||
The inspectors observed selected plant testing and other power ascension activities during the implementation of the (2350 MWt to 2644 MWt) extended power uprate. The inspectors observed control room and in-plant acvitities during the ascension to the new 100% power level at various plateau levels, and walked down plant systems to ensure adverse conditions were both identified, and if warranted, entered into the corrective action program of resolution. | The inspectors observed selected plant testing and other power ascension activities during the implementation of the (2350 MWt to 2644 MWt) extended power uprate. The inspectors observed control room and in-plant acvitities during the ascension to the new 100% power level at various plateau levels, and walked down plant systems to ensure adverse conditions were both identified, and if warranted, entered into the corrective action program of resolution. | ||
* Observed power escalation from 235 MWe to 239 MWe over one hour in accordance with licensee procedure 3-GOP-301, Hot Standby to Power Operations The inspectors also reviewed operator actions, applicable procedure changes, and reviewed selected plant design changes and other inspection activities conducted under the normal baseline inspection program, to ensure an adequate sample of risk-significant attributes required by the governing procedure were evaluated. This included changes to plant emergency operating procedure, as well as associated operator briefings and training to address those actions resulting from a revised steam generator tube rupture analysis. | * Observed power escalation from 235 MWe to 239 MWe over one hour in accordance with licensee procedure 3-GOP-301, Hot Standby to Power Operations | ||
The inspectors also reviewed operator actions, applicable procedure changes, and reviewed selected plant design changes and other inspection activities conducted under the normal baseline inspection program, to ensure an adequate sample of risk-significant attributes required by the governing procedure were evaluated. This included changes to plant emergency operating procedure, as well as associated operator briefings and training to address those actions resulting from a revised steam generator tube rupture analysis. | |||
====b. Findings==== | ====b. Findings==== | ||
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====a. Inspection Scope==== | ====a. Inspection Scope==== | ||
Leakage from buried and underground pipes has resulted in ground water contamination incidents with associated heightened NRC and public interest. The industry issued a guidance document, Nuclear Energy Institute (NEI) 09-14, "Guideline for the Management of Buried Piping Integrity," (ADAMS Accession No. ML1030901420), to describe the goals and required actions (commitments made by the licensee) resulting from this underground piping and tank initiative. On December 31, 2010, NEI issued Revision 1 to NEI 09-14, "Guidance for the Management of Underground Piping and Tank Integrity," (ADAMS Accession No. ML110700122), with an expanded scope of components which included underground piping that was not in direct contact with the soil and underground tanks. On November 17, 2011, the NRC issued TI-2515/182 "Review of the Industry Initiative to Control Degradation of Underground Piping and Tanks," to gather information related to the industry's implementation of this initiative. | Leakage from buried and underground pipes has resulted in ground water contamination | ||
incidents with associated heightened NRC and public interest. The industry issued a guidance document, Nuclear Energy Institute (NEI) 09-14, "Guideline for the Management of Buried Piping Integrity," (ADAMS Accession No. ML1030901420), to describe the goals and required actions (commitments made by the licensee) resulting from this underground piping and tank initiative. On December 31, 2010, NEI issued Revision 1 to NEI 09-14, "Guidance for the Management of Underground Piping and Tank Integrity," (ADAMS Accession No. ML110700122), with an expanded scope of components which included underground piping that was not in direct contact with the soil and underground tanks. On November 17, 2011, the NRC issued TI-2515/182 "Review of the Industry Initiative to Control Degradation of Underground Piping and Tanks," to gather information related to the industry's implementation of this initiative. | |||
The inspectors reviewed the licensee's programs for buried pipe and underground piping and tanks in accordance with TI-2515/182 to determine if the program attributes and completion dates identified in Sections 3.3 A and 3.3 B of NEI 09-14, Revision 1 were contained in the licensee's program and implementing procedures. For the buried pipe and underground piping program attributes, with completion dates that had passed, the inspectors reviewed records to determine if the attribute was in fact complete and to determine if the attribute was accomplished in a manner which reflected good or poor practices in program management. | The inspectors reviewed the licensee's programs for buried pipe and underground piping and tanks in accordance with TI-2515/182 to determine if the program attributes and completion dates identified in Sections 3.3 A and 3.3 B of NEI 09-14, Revision 1 were contained in the licensee's program and implementing procedures. For the buried pipe and underground piping program attributes, with completion dates that had passed, the inspectors reviewed records to determine if the attribute was in fact complete and to determine if the attribute was accomplished in a manner which reflected good or poor practices in program management. | ||
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* The area appears to be free of potentially adverse seismic interactions that could cause flooding or spray in the area | * The area appears to be free of potentially adverse seismic interactions that could cause flooding or spray in the area | ||
* The area appears to be free of potentially adverse seismic interactions that could cause a fire in the area | * The area appears to be free of potentially adverse seismic interactions that could cause a fire in the area | ||
* The area appears to be free of potentially adverse seismic interactions associated with housekeeping practices, storage of portable equipment, and temporary installations (e.g., scaffolding, lead shielding) | * The area appears to be free of potentially adverse seismic interactions associated with housekeeping practices, storage of portable equipment, and temporary installations (e.g., scaffolding, lead shielding) | ||
Additionally, inspectors verified that items that could allow the spent fuel pool to drain down rapidly were added to the Seismic Walkdown Equipment List (SWEL) and these items were walked down by the licensee. | Additionally, inspectors verified that items that could allow the spent fuel pool to drain down rapidly were added to the Seismic Walkdown Equipment List (SWEL) and these items were walked down by the licensee. | ||
| Line 461: | Line 588: | ||
==4OA6 Meetings, Including Exit== | ==4OA6 Meetings, Including Exit== | ||
===Exit Meeting Summary=== | |||
The resident inspectors presented the inspection results to Mr. Kiley and other members of licensee management on January 16, 2013. The inspectors asked the licensee whether any of the material examined during the inspection should be considered proprietary information. The licensee did not identify any proprietary information. | The resident inspectors presented the inspection results to Mr. Kiley and other members of licensee management on January 16, 2013. The inspectors asked the licensee whether any of the material examined during the inspection should be considered proprietary information. The licensee did not identify any proprietary information. | ||
ATTACHMENT: | ATTACHMENT: SUPPPL EMENTAL INFORMATION | ||
=SUPPLEMENTAL INFORMATION= | =SUPPLEMENTAL INFORMATION= | ||
| Line 502: | Line 630: | ||
===Opened and Closed=== | ===Opened and Closed=== | ||
: 05000251, 2012005-01 FIN Failure to Verify 1B Feedwater Heater Drain Valve Closed (Section 1R11.2) | : 05000251, 2012005-01 FIN Failure to Verify 1B Feedwater Heater Drain Valve Closed (Section 1R11.2) | ||
===Closed=== | ===Closed=== | ||
: 05000250, 251/2515/188 TI Inspection of Near-Term Task Force Recommendation 2.3 Seismic Walkdowns (Section 4OA5.4) | : 05000250, 251/2515/188 TI Inspection of Near-Term Task Force Recommendation 2.3 Seismic Walkdowns (Section | ||
: 4OA5.4) | |||
: Attachment | : Attachment | ||
: [[Closes LER::05000250/LER-2012-003]]-00 LER Condition Prohibited by Technical Specifications Due to Instrument Valve Mispositioning (Section 4OA3.1) | : [[Closes LER::05000250/LER-2012-003]]-00 LER Condition Prohibited by Technical Specifications Due to Instrument Valve Mispositioning (Section | ||
: 4OA3.1) | |||
: [[Closes LER::05000250/LER-2012-004]]-00 LER Condition Prohibited by Technical Specifications Due to Instrument Process Line Reversal During | : [[Closes LER::05000250/LER-2012-004]]-00 LER Condition Prohibited by Technical Specifications Due to Instrument Process Line Reversal During | ||
: Replacement (Section 4OA3.2) | : Replacement (Section 4OA3.2) | ||
===Discussed=== | ===Discussed=== | ||
: 05000250, 251/2515/182 TI Temporary Instruction (TI) -2515/182 - Review of the Implementation of the Industry Initiative to Control Degradation of Underground Piping and Tanks, Phase 1 (Section 4OA5.3) | : 05000250, 251/2515/182 TI Temporary Instruction (TI) -2515/182 - Review of the Implementation of the Industry Initiative to Control Degradation of Underground Piping and Tanks, Phase 1 (Section 4OA5.3) | ||
==LIST OF DOCUMENTS REVIEWED== | ==LIST OF DOCUMENTS REVIEWED== | ||
==Section 1R08: Inservice Inspection (ISI) Activities Corrective Action | ==Section 1R08: Inservice Inspection (ISI) Activities== | ||
: Corrective Action | |||
: AR 01830766 | : AR 01830766 | ||
: AR 01831425 | : AR 01831425 | ||
| Line 528: | Line 661: | ||
: AR 1823799 | : AR 1823799 | ||
: AR 1823915 | : AR 1823915 | ||
: AR 2008-14563 | : AR 2008-14563 | ||
===Procedures=== | ===Procedures=== | ||
: Areva Document # 03-1246524, Instructions for Plug Inspection, Rev. 11 | : Areva Document # 03-1246524, Instructions for Plug Inspection, Rev. 11 | ||
: Areva Document # 51-5029214-10 Qualified Eddy Current Techniques for Turkey Point (PTN) Units 3 & 4 Areva Examination Technique Specification Sheet 1 for | : Areva Document # 51-5029214-10 Qualified Eddy Current Techniques for Turkey Point (PTN) | ||
: Units 3 & 4 Areva Examination Technique Specification Sheet 1 for | |||
: PTN4-EOC26 Rev. 0 | : PTN4-EOC26 Rev. 0 | ||
: Areva Examination Technique Specification Sheet 2 for | : Areva Examination Technique Specification Sheet 2 for | ||
| Line 553: | Line 687: | ||
===Other Documents=== | ===Other Documents=== | ||
: 0-ADM-537, Boric Acid Corrosion Control Program, Rev. 6 Areva Document # 03-9195093, Florida Power and Light Turkey Point Unit 4 Secondary Side Inspection On-Site Report, Rev. 0 Areva Personnel Certification, D. Austin Areva Personnel Certification, G. Chapman Areva Personnel Certification, T. Allen Bonney Forge CMTR No. | : 0-ADM-537, Boric Acid Corrosion Control Program, Rev. 6 Areva Document # 03-9195093, Florida Power and Light Turkey Point Unit 4 Secondary Side Inspection On-Site Report, Rev. 0 Areva Personnel Certification, D. Austin Areva Personnel Certification, G. Chapman Areva Personnel Certification, T. Allen Bonney Forge CMTR No. | ||
: 311480, Heat No. 44027 Boric Acid Corrosion Control Program Quick | : 311480, Heat No. 44027 | ||
: Boric Acid Corrosion Control Program Quick Ho | |||
t Self Assessment Plan and Report, 8/1-30/2011 Curtis Wright Personnel Certification, J. Timm Curtis Wright Personnel Certification, K. Nelson Curtis Wright Personnel Certification, T. Moore General Electric UT Probe Certificate of Conformity, S/N SI0071 | |||
: Ladish Valves CMTR No. | |||
: 1003598 Lambert Macgill Thomas Personnel Certification, B. Kissack Lambert Macgill Thomas Personnel Certification, J. Fuller Lambert Macgill Thomas Personnel Certification, M. Shoemaker Magnaflux Dual Purpose Penetrant Batch No. | : 1003598 Lambert Macgill Thomas Personnel Certification, B. Kissack Lambert Macgill Thomas Personnel Certification, J. Fuller Lambert Macgill Thomas Personnel Certification, M. Shoemaker Magnaflux Dual Purpose Penetrant Batch No. | ||
: 965028 Certification Magnaflux Spotcheck Developer Batch No. 08F02K, 08M01K Certification Panametrics/Epoch 4 UT Instrument Linearity Record, S/N | : 965028 Certification Magnaflux Spotcheck Developer Batch No. 08F02K, 08M01K Certification Panametrics/Epoch 4 UT Instrument Linearity Record, S/N | ||
| Line 567: | Line 704: | ||
: Attachment | : Attachment | ||
==Section 1EP4: Emergency Action Level and Emergency Plan Changes Change Packages Radiological Emergency Plan, Revisions 54 and 55 | ==Section 1EP4: Emergency Action Level and Emergency Plan Changes== | ||
: Change Packages Radiological Emergency Plan, Revisions 54 and 55 | |||
: 0-EPIP-20126, "Off-site Dose Calculations," Revision 1 | : 0-EPIP-20126, "Off-site Dose Calculations," Revision 1 | ||
: 0-EPIP-20132, "Technical Support Center (TSC) Activation and Operation," Revision 2A | : 0-EPIP-20132, "Technical Support Center (TSC) Activation and Operation," Revision 2A | ||
| Line 575: | Line 713: | ||
: Radiological Hazard Assessment and Exposure Controls | : Radiological Hazard Assessment and Exposure Controls | ||
===Procedures=== | ===Procedures=== | ||
and Guidance Documents 0-ADM-023, Inventory Control and Accounting of Radioactive Sources, Rev. 2 | and Guidance Documents | ||
: 0-HPA-001, Radiation Work Permit Initiation and Termination, Rev. 3 0-ADM-600, Radiation Protection Manual, Rev. 1 0-ADM-605, Control of Radioactive Material, Rev. 1 | : 0-ADM-023, Inventory Control and Accounting of Radioactive Sources, Rev. 2 | ||
: 0-HPA-001, Radiation Work Permit Initiation and Termination, Rev. 3 | |||
: 0-ADM-600, Radiation Protection Manual, Rev. 1 | |||
: 0-ADM-605, Control of Radioactive Material, Rev. 1 | |||
: 0-HPA-031.2, Multibadge Exposure Monitoring, 0A | : 0-HPA-031.2, Multibadge Exposure Monitoring, 0A | ||
: 0-HPS-021.3, Identification, Survey, and Release of Material for Unrestricted Use, Rev. 4 | : 0-HPS-021.3, Identification, Survey, and Release of Material for Unrestricted Use, Rev. 4 | ||
: RP-AA-100-1001, Radiation Protection Conduct of Operations Guideline, Rev. 1 | : RP-AA-100-1001, Radiation Protection Conduct of Operations Guideline, Rev. 1 | ||
: RP-AA-101-2004, Method for Monitoring and Assigning Effective Dose Equivalent (EDE) for | : RP-AA-101-2004, Method for Monitoring and Assigning Effective Dose Equivalent (EDE) for High Dose Gradient Work, Rev. 2 | ||
: RP-SR-101-1003, Personnel Contamination Monitoring and Decontamination, Rev. 3 | : RP-SR-101-1003, Personnel Contamination Monitoring and Decontamination, Rev. 3 | ||
: RP-SR-102-1001, Area Radiological Surveys and Analysis, Rev. 2 | : RP-SR-102-1001, Area Radiological Surveys and Analysis, Rev. 2 | ||
| Line 589: | Line 729: | ||
: RP-TP-103-1003, RP Survey Requirements for Extended Power Uprate Secondary Side | : RP-TP-103-1003, RP Survey Requirements for Extended Power Uprate Secondary Side | ||
: Components and Material, Rev. 0A | : Components and Material, Rev. 0A | ||
: RP-TP-107-1001, Storage of Highly Radioactive Material in the Reactor Cavity or Spent Fuel Pool, Rev. 0 | : RP-TP-107-1001, Storage of Highly Radioactive Material in the Reactor Cavity or Spent Fuel | ||
: Pool, Rev. 0 | |||
: Records and Data Reviewed Quick Hit Self-Assessment, "Crud Burst Control Self Assessment," 02/24/12 | : Records and Data Reviewed Quick Hit Self-Assessment, "Crud Burst Control Self Assessment," 02/24/12 | ||
: Turkey Point Nuclear Oversight Report, | : Turkey Point Nuclear Oversight Report, | ||
| Line 610: | Line 751: | ||
: ACS, A/S Log Ref No. P0-12-6550, U4 RCB Rx Sump Outside, Dated 12/12/12 | : ACS, A/S Log Ref No. P0-12-6550, U4 RCB Rx Sump Outside, Dated 12/12/12 | ||
: ACS, A/S Log Ref No. P0-12-6517, U4 RCB Rx Sump General Area, Dated 12/12/12 | : ACS, A/S Log Ref No. P0-12-6517, U4 RCB Rx Sump General Area, Dated 12/12/12 | ||
: HP-44:76, Survey Log No. 12-12406, Unit-4 'A' Steam Generator, Dated 12/04/12 | : HP-44:76, Survey Log No. 12-12406, Unit-4 | ||
'A' Steam Generator, Dated 12/04/12 | |||
: HP-44:76, Survey Log No. 12-12420, Unit-4 'C' Steam Generator, Dated 12/04/12 | : HP-44:76, Survey Log No. 12-12420, Unit-4 'C' Steam Generator, Dated 12/04/12 | ||
: HP-47:48, Survey Log No. 12-12917, Unit-4 'C' Steam Generator, Dated 12/11/12 | : HP-47:48, Survey Log No. 12-12917, Unit-4 'C' Steam Generator, Dated 12/11/12 | ||
| Line 626: | Line 768: | ||
: RWP No. 12-4024, Bottom Mounted Instrumentation Project (BMI), Rev. 3 | : RWP No. 12-4024, Bottom Mounted Instrumentation Project (BMI), Rev. 3 | ||
: RWP No. 12-4102, U4R27 Thimble Tube Replacement Work on 58', Rev 2 RWP No. 12-4205, Outage Locked High Radiation Area Work, Rev 3 SEN0016A- RWP and Task Descriptions, Dated 11/19/12 | : RWP No. 12-4102, U4R27 Thimble Tube Replacement Work on 58', Rev 2 RWP No. 12-4205, Outage Locked High Radiation Area Work, Rev 3 SEN0016A- RWP and Task Descriptions, Dated 11/19/12 | ||
: Corrective Action Program (CAP) Documents Action Request (AR) | : Corrective Action Program (CAP) Documents | ||
===Action Request=== | |||
(AR) | |||
: 1702878, Alpha Contamination Issues | : 1702878, Alpha Contamination Issues | ||
: AR 01824368, Review of TLD Separations | : AR 01824368, Review of TLD Separations | ||
| Line 637: | Line 781: | ||
: CS-137 Source S/N 72504 is Leaking Unable to Perform PM | : CS-137 Source S/N 72504 is Leaking Unable to Perform PM | ||
: AR 01774679, RWP Radiation Setpoints Very High | : AR 01774679, RWP Radiation Setpoints Very High | ||
: AR 01712443, Radiation Area Boundary Greater Than 5 Mr/Hr | : AR 01712443, Radiation Area Boundary Greater Than 5 Mr/Hr Section 2RS08: | ||
: Radioactive Solid Waste Processing and Radioactive Material Handling, Storage, and Transportation | : Radioactive Solid Waste Processing and Radioactive Material Handling, Storage, and Transportation | ||
===Procedures=== | ===Procedures=== | ||
and Guidance Documents Administrative Procedure (ADM)-605, Control of Radioactive Material, Revision (Rev.) 1 | and Guidance Documents | ||
: Administrative Procedure (ADM)-605, Control of Radioactive Material, Revision (Rev.) 1 | |||
: Florida Power & Light, Turkey Point Nuclear Station Nuclear Training Department, Lesson Package Number (No.) | : Florida Power & Light, Turkey Point Nuclear Station Nuclear Training Department, Lesson Package Number (No.) | ||
: 2400080,Radioactive Material Shipping, 08/31/11 0-HPA-045, Process Control Program, Rev. 0 | : 2400080,Radioactive Material Shipping, 08/31/11 0-HPA-045, Process Control Program, Rev. 0 | ||
| Line 650: | Line 794: | ||
: DTS-WPS Media Sluice, Rev. 1 0-NCOP-502, DTS Media Dewatering, 5/20/10 | : DTS-WPS Media Sluice, Rev. 1 0-NCOP-502, DTS Media Dewatering, 5/20/10 | ||
: 0-HPS-040.5, 10 CFR61 Compliance and Radioactive Waste/Material Shipment Classification and Characterization, 06/22/10 | : 0-HPS-040.5, 10 CFR61 Compliance and Radioactive Waste/Material Shipment Classification and Characterization, 06/22/10 | ||
: Records and Data Reviewed | : Records and Data Reviewed Radioactive Waste Manifest Tracking Log, Calendar Year (CY) 2011 and Year-to-Date (YTD) | ||
: 2012 | : 2012 | ||
: Radioactive Material Shipment Tracking Log, Calendar Year (CY) 2011 and Year-to-Date (YTD) | : Radioactive Material Shipment Tracking Log, Calendar Year (CY) 2011 and Year-to-Date (YTD) | ||
: 2012 | : 2012 | ||
: Radioactive Material Shipment (M)-12-149, UN3321, Radioactive material, low specific activity(LSA-II), 7 Fissile Excepted, 1 Metal Box UniTech Used Material 40' SeaLand | : Radioactive Material Shipment (M)-12-149, UN3321, Radioactive material, low specific activity(LSA-II), 7 Fissile Excepted, 1 Metal Box UniTech Used Material 40' SeaLand Container, 12/12/12 | ||
: Radioactive Waste Shipment, (W)-12-043, UN3321, Radioactive material, low specific activity(LSA-II), 7 Fissile Excepted, 2 Metal Boxes 2012, Dry Active Waste (DAW), 12/12/12 | : Radioactive Waste Shipment, (W)-12-043, UN3321, Radioactive material, low specific activity(LSA-II), 7 Fissile Excepted, 2 Metal Boxes 2012, Dry Active Waste (DAW), 12/12/12 | ||
: Radioactive Waste Shipment, W-12-029, UN3321, Radioactive material, low specific activity (LSA-II), 7 Fissile Excepted, 2 Metal Boxes, 2012 DAW, 07/26/12 Radioactive Waste Shipment, W-12-028, UN3321, Radioactive material, low specific activity(LSA-II), 7 Fissile Excepted, 1 Metal Box, 2012 DAW, 1 Metal Box | : Radioactive Waste Shipment, W-12-029, UN3321, Radioactive material, low specific activity (LSA-II), 7 Fissile Excepted, 2 Metal Boxes, 2012 DAW, 07/26/12 Radioactive Waste Shipment, W-12-028, UN3321, Radioactive material, low specific activity(LSA-II), 7 Fissile Excepted, 1 Metal Box, 2012 DAW, 1 Metal Box | ||
| Line 664: | Line 806: | ||
: 07/12/12 Radioactive Material Shipment, M-12-091, UN3321, Radioactive material, low specific activity(LSA-II), 7 Fissile Excepted, 1 Metal Box AREVA | : 07/12/12 Radioactive Material Shipment, M-12-091, UN3321, Radioactive material, low specific activity(LSA-II), 7 Fissile Excepted, 1 Metal Box AREVA | ||
: 9011352, 06/28/12 | : 9011352, 06/28/12 | ||
: Radioactive Material Shipment, M-12-069, UN3321, Radioactive material, low specific activity(LSA-II), 7 Fissile Excepted, 1 Metal Box UniTech Used Material, 40' SeaLand | : Radioactive Material Shipment, M-12-069, UN3321, Radioactive material, low specific activity(LSA-II), 7 Fissile Excepted, 1 Metal Box UniTech Used Material, 40' SeaLand Container, 05/26/12 Radioactive Material Shipment, M-12-006, UN3321, Radioactive material, low specific activity(LSA-II), 7 Fissile Excepted, 1 Metal Box, Spent Fuel Pool Handling Tool, 02/17/12 | ||
: CFR Part 61 Analysis for 2012 Dry Active Waste (DAW), 07/16/2012 | : CFR Part 61 Analysis for 2012 Dry Active Waste (DAW), 07/16/2012 | ||
: CFR Part 61 Analysis for 2012 Unit 3 Reactor Sump DAW, 07/16/2012 | : CFR Part 61 Analysis for 2012 Unit 3 Reactor Sump DAW, 07/16/2012 | ||
| Line 674: | Line 815: | ||
: CV-3-4658A will not go to close | : CV-3-4658A will not go to close | ||
: WR 94036557, | : WR 94036557, | ||
: LCV-4-1003B limit switch shows closed when valve is open Corrective Action Program (CAP) Documents Turkey Point Nuclear Oversight Report No. | : LCV-4-1003B limit switch shows closed when valve is open | ||
: Corrective Action Program (CAP) Documents Turkey Point Nuclear Oversight Report No. | |||
: PTN-12-002, Radiological Protection and Radwaste, | : PTN-12-002, Radiological Protection and Radwaste, | ||
: 03/15/2012 | : 03/15/2012 | ||
| Line 682: | Line 824: | ||
: AR 01772330, Radioactive shipment egress prevented by west end of NAB | : AR 01772330, Radioactive shipment egress prevented by west end of NAB | ||
: AR 01770861, RWST waste seal and will require additional handling prior to shipment Attachment | : AR 01770861, RWST waste seal and will require additional handling prior to shipment Attachment | ||
: AR 01715311, Informational radiological posting not removed from non-radiologically | : AR 01715311, Informational radiological posting not removed from non-radiologically contaminated equipment | ||
: AR 01700085, Delay in receipt of radioactive material shipment, | : AR 01700085, Delay in receipt of radioactive material shipment, | ||
: AR 1747168, Initial Cavity survey After Draining | : AR 1747168, Initial Cavity survey After Draining | ||
| Line 688: | Line 830: | ||
: AR 1823307, Boilermaker Moved Locked HRA Sign | : AR 1823307, Boilermaker Moved Locked HRA Sign | ||
: AR 1788351, Inadequate HRA Postings | : AR 1788351, Inadequate HRA Postings | ||
: AR 1752780, Individual Did Not Acknowledge Dose Rate Alarm on Sentinel | : AR 1752780, Individual Did Not Acknowledge Dose Rate Alarm on Sentinel | ||
===Procedures=== | ===Procedures=== | ||
and Guidance Documents 0-ADM-032, NRC Performance Indicators Turkey Point, Rev. 4 | and Guidance Documents | ||
: Records and Data Reviewed | : 0-ADM-032, NRC Performance Indicators Turkey Point, Rev. 4 | ||
: Records and Data Reviewed Annual Radioactive Effluent Release Report, January 2011 through December 2011 | |||
: AR 01643894, Documentation of unplanned release | : AR 01643894, Documentation of unplanned release | ||
: AR 01687974, Inability to close liquid release L-2011-111 B-MT | : AR 01687974, Inability to close liquid release L-2011-111 B-MT | ||
: Annual Radioactive Effluent Release Report Gaseous Effluent, Site Ground Releases, as of | : Annual Radioactive Effluent Release Report Gaseous Effluent, Site Ground Releases, as of December 12, 2012 0-NCOP-006, Gas Gamma Beta Dose Summary Sheet, December 2011 | ||
: 0-NCOP-006, Liquid Dose Summary Sheet, December 2011 | : 0-NCOP-006, Liquid Dose Summary Sheet, December 2011 | ||
: 0-NCOP-006, Gas Gamma Beta Dose Summary Sheet, November 2012 | : 0-NCOP-006, Gas Gamma Beta Dose Summary Sheet, November 2012 | ||
: 0-NCOP-006, Liquid Dose Summary Sheet, November 2012 | : 0-NCOP-006, Liquid Dose Summary Sheet, November 2012 | ||
: PTN Quarterly PI Reports, Dated | : PTN Quarterly PI Reports, Dated 2 | ||
nd Qtr 2011 to September 2012 List of Dose and Dose Rate alarms for the periods 04/02/11 - 11/20/12 Exposure Investigation Reports, dated from 04/01/11 through 12/12/12 | |||
: Section 4OA5.1: | : Section 4OA5.1: | ||
: Temporary Instruction 2515/182 Procedures | : Temporary Instruction 2515/182 | ||
===Procedures=== | |||
: ER-AA-102, Buried Piping Program, Rev. 1 | : ER-AA-102, Buried Piping Program, Rev. 1 | ||
: ER-AA-102-1000, Buried Piping Examination Procedure, Rev. 01 | : ER-AA-102-1000, Buried Piping Examination Procedure, Rev. 01 | ||
| Line 718: | Line 861: | ||
: Buried Piping Program Health Report, 3 Quarter 2012 Buried Piping Program Health Report, 4 Quarter 2011 | : Buried Piping Program Health Report, 3 Quarter 2012 Buried Piping Program Health Report, 4 Quarter 2011 | ||
: NEI 09-14 Prioritization of Underground Piping, June 2012 | : NEI 09-14 Prioritization of Underground Piping, June 2012 | ||
: Attachment Quick Hit Self Assessment Report, 2011 Fleet Buried Piping Program Self-Assessment, 10/3/2011 Quick Hit Self Assessment Report, QHSA for NRC Buried Piping Inspection | : Attachment Quick Hit Self Assessment Report, 2011 Fleet Buried Piping Program Self-Assessment, 10/3/2011 | ||
: TI-182, September 14-19, 2012 Report No. | : Quick Hit Self Assessment Report, QHSA for NRC Buried Piping Inspection | ||
: TI-182, September | |||
: 14-19, 2012 Report No. | |||
: 1016456, Recommendation for an Effective Program to Control Degradation of Buried Piping, December 2008 Schedule for Buried and Underground Piping Examinations Turkey Point Buried Piping Program Basis Document, Revision 0 Turkey Point Power Station Underground Piping and Tanks Examination Plan, Rev. 0 | : 1016456, Recommendation for an Effective Program to Control Degradation of Buried Piping, December 2008 Schedule for Buried and Underground Piping Examinations Turkey Point Buried Piping Program Basis Document, Revision 0 Turkey Point Power Station Underground Piping and Tanks Examination Plan, Rev. 0 | ||
: Unit 3 Circulating Water Pipe NDE Inspection, August 2012 | : Unit 3 Circulating Water Pipe NDE Inspection, August 2012 | ||
: Section 4OA5.4: | : Section 4OA5.4: | ||
: Temporary Instruction 2515/188 EPRI | : Temporary Instruction 2515/188 | ||
: EPRI | |||
: 1025286 "Seismic Walkdown Guidance for Resolution of Fukushima Near-Term Task Force Recommendation 2.3 Turkey Point Seismic Walkdown Equipment List (SWEL) 1 and 2 | : 1025286 "Seismic Walkdown Guidance for Resolution of Fukushima Near-Term Task Force Recommendation 2.3 Turkey Point Seismic Walkdown Equipment List (SWEL) 1 and 2 | ||
: Various Seismic Evaluation Training Course Certifications Area Walk-By Checklist and Seismic Walkdown Checklist for Areas 347 and 368 | : Various Seismic Evaluation Training Course Certifications Area Walk-By Checklist and Seismic Walkdown Checklist for Areas 347 and 368 | ||
}} | }} | ||
Revision as of 07:26, 19 July 2018
| ML13030A208 | |
| Person / Time | |
|---|---|
| Site: | Turkey Point |
| Issue date: | 01/30/2013 |
| From: | Sandal S R NRC/RGN-II/DRP/RPB3 |
| To: | Nazar M Florida Power & Light Co |
| References | |
| IR-12-005 | |
| Preceding documents: |
|
| Download: ML13030A208 (39) | |
Text
January 30, 2013
Mr. Mano Nazar Executive Vice President and Chief Nuclear Officer Florida Power and Light Company P.O. Box 14000 Juno Beach, FL 33408-0420
SUBJECT: TURKEY POINT NUCLEAR PLANT - NRC INTEGRATED INSPECTION REPORT 05000250/2012005 AND 05000251/2012005
Dear Mr. Nazar:
On December 31, 2012, the US Nuclear Regulatory Commission (NRC) completed an inspection at your Turkey Point Nuclear Plant Units 3 and 4. The enclosed integrated inspection report documents the inspection findings, which were discussed on January 16, 2013, with Mr.
Kiley and other members of your staff.
The inspection examined activities conducted under your license as they relate to safety and compliance with the Commission's rules and regulations and with the conditions of your license.
The inspectors reviewed selected procedures and records, observed activities, and interviewed personnel.
One self-revealing finding of very low safety significance (Green) was identified during this inspection. This finding did not involve a violation of NRC regulatory requirements.
If you disagree with a cross-cutting aspect assignment in this report, you should provide a response within 30 days of the date of this report, with the basis of your disagreement, to the Regional Administrator, Region II and the NRC Resident Inspector at Turkey Point Nuclear Plant. In accordance with 10 CFR 2.790 of the NRC's "Rules of Practice", a copy of this letter, its enclosure, and your response (if any) will be available electronically for public inspection in the NRC Public Document Room or from the Publicly Available Records (PARS) component of NRC's document system (ADAMS). ADAMS is accessible from the NRC Website at http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room).
Sincerely,/RA/ Shane Sandal, Acting Chief Reactor Projects Branch 3 Division of Reactor Projects
Docket Nos: 50-250, 50-251 License Nos: DPR-31, DPR-41
Enclosure:
Inspection Report 05000250/2012005, 05000251/2012005
w/Attachment:
Supplemental Information cc w/encl: (See page 3)
_________________________ X SUNSI REVIEW COMPLETE G FORM 665 ATTACHED OFFICE RII:DRP RII:DRP RII:DRS RII:DRS RII:DRP RII:DRS RII:DRS RII:DRS SIGNATURE Via email Via email Via email Via email Via email Via email Via email Via email NAME JStewart THoeg PCapehart CFletcher MBarillas AVargas MCoursey WPursley DATE 01/22/2013 01/23/2013 01/22/2013 01/22/2013 01/22/2013 01/23/2013 01/22/2013 01/22/2013 E-MAIL COPY? YES NO YES NO YES NO YES NO YES NO YES NO YES NO YES NO OFFICE RII:DRS RII:DRS NRR RII:DRS NRR RII:DRP RII:DRP SIGNATURE Via email Via email Via email via email /BRB for/ Via email MJR /RA/ SRS /RA/ NAME RTaylor DMas AZoulis GKuzo JLaughlin MRiches SSandal DATE 01/22/2013 01/22/2013 01/22/2013 01/23/2013 01/28/2013 01/28/2013 01/30/2013 E-MAIL COPY? YES NO YES NO YES NO YES NO YES NO YES NO 3
cc w/encl:
Alison Brown Nuclear Licensing
Florida Power & Light Company Electronic Mail Distribution
Larry Nicholson Director Licensing
Florida Power & Light Company Electronic Mail Distribution
Michael Kiley Site Vice President
Turkey Point Nuclear Plant Florida Power and Light Company Electronic Mail Distribution Niel Batista Emergency Management Coordinator Department of Emergency Management and Homeland Security Electronic Mail Distribution Paul Freeman Vice President Organizational Effectiveness
Florida Power & Light Company Electronic Mail Distribution
Peter Wells Vice President
Outage Support CFAM
Florida Power & Light Company Electronic Mail Distribution
Robert J. Tomonto Licensing Manager
Turkey Point Nuclear Plant Florida Power & Light Company Electronic Mail Distribution
Eric McCartney
Plant General Manager
Turkey Point Nuclear Plant Florida Power and Light Company Electronic Mail Distribution
Cynthia Becker (Acting) Chief Florida Bureau of Radiation Control Department of Health Electronic Mail Distribution
Attorney General Department of Legal Affairs The Capitol PL-01 Tallahassee, FL 32399-1050
James Petro Managing Attorney-Nuclear Florida Power & Light Company Electronic Mail Distribution
County Manager of Miami-Dade County 111 NW 1st Street, 29th Floor Miami, FL 33128
George Gretsas City Manager City of Homestead Electronic Mail Distribution 4
Letter to Mano Nazar from Shane Sandal dated January 30, 2013
SUBJECT: TURKEY POINT NUCLEAR PLANT - NRC INTEGRATED INSPECTION REPORT 05000250/2012005 AND 05000251/2012005
Distribution w/encl
- C. Evans, RII L. Douglas, RII OE Mail RIDSNRRDIRS PUBLIC RidsNrrPMTurkeyPoint Resource Enclosure U.S. NUCLEAR REGULATORY COMMISSION REGION II Docket Nos.: 50-250, 50-251
Report No: 05000250/2012005, 05000251/2012005
Licensee: Florida Power & Light Company (FPL)
Facility: Turkey Point Nuclear Plant, Units 3 & 4
Location: 9760 S. W. 344th Street Homestead, FL 33035
Dates: October 1, 2012 to December 31, 2012
Inspectors: J. Stewart, Senior Resident Inspector T. Hoeg, Senior Resident Inspector P. Capehart, Senior Operations Engineer C. Fletcher, Senior Reactor Inpsector M. Barillas, Resident Inspector A. Vargas, Reactor Inspector M. Coursey, Reactor Inspector
R. Taylor, Senior Project Engineer D. Mas-Penaranda, Project Engineer A. Zoulis, Senior Risk Analyst J. Laughlin, Emergency Preparedness Inspector G. Kuzo, Senior Health Physicist W. Pursley, Health Physicist Approved by: S. Sandal, Acting Chief Reactor Projects Branch 3
Division of Reactor Projects Enclosure
SUMMARY OF FINDINGS
IR 05000250/2012005, 05000251/2012005; 10/01/2012 - 12/31/2012; Turkey Point Nuclear Power Plant, Units 3 and 4; Licensed Operator Requalification Program
The report covered a three month period of inspection by resident inspectors and region based inspectors. One Green Finding was identified. The significance of inspection findings are identified by their color i.e. (greater than Green, or Green, White, Yellow, or Red) and determined using Inspection Manual Chapter (IMC) 0609, "Significance Determination Process" (SDP) dated June 2, 2011. The cross-cutting aspect was determined using IMC 310, Components Within the Cross-Cutting Areas" dated October 28, 2011. All violations of NRC requirements are dispositioned in accordance with the NRC's Enforcement Policy dated June 7, 2012. The NRC's program for overseeing the safe operation of commercial nuclear power reactors is described in NUREG-1649, "Reac tor Oversight Process," Revision 4.
Cornerstone: Initiating Events
- Green: A self-revealing finding was identified when the licensee failed to follow procedure 0-ADM-222, Drain and Vent Rig Controls, while installing a temporary drain hose on Turkey Point Unit 4 in-service equipment. Operations and maintenance workers failed to verify a drain line flow path was isolated on the 1B feed water heater prior to removing a pipe valve cap that resulted in an unexpected lowering of condenser vacuum. Operators took action to close the open drain line isolation valve and terminate the plant transient. The licensee captured this condition in their corrective action program as AR 1819010.
The licensee's failure to verify the closed position of 1B feed water heater drain valve 4-30-128, as required by procedure 0-ADM-222, prior to removing the pipe cap was a performance deficiency. The inspectors determined the performance deficiency was more than minor using IMC 0612, Appendix B, Issue Screening, because the performance deficiency was associated with the configuration control attribute of the initiating events cornerstone, and adversely affected the cornerstone objective to limit the likelihood of events that upset plant stability and challenge critical safety functions during power operations. Specifically, the failure to verify the position of 4-30-128 resulted in lowering condenser vacuum that could have led to a reactor trip and the unavailability of the main condenser. The inspectors evaluated the finding using the significance determination process for findings at power of IMC 0609, Appendix A,
Exhibit 1, Transient Initiators. The inspectors determined the finding was of very low safety significance (Green) because the finding did not result in a reactor trip and a loss of mitigation equipment relied upon to transition the plant to a stable shutdown condition.
The finding was associated with a cross-cutting aspect in the work practices component of the human performance area because the licensee did not define and effectively communicate expectations, or follow the procedural requirement to physically verify valve position during the drain hose installation work H.4(b). (Section 1R11.2)
REPORT DETAILS
Summary of Plant Status
- Unit 3 began the period at 29 percent power while adjustments were made to secondary plant chemistry. Unit 3 reached full power on November 16, 2012, where they remained through the remainder of this inspection period.
Unit 4 began this inspection period at full power. On November 4, 2012, reactor power was reduced to 30 percent to support secondary plant testing. On November 5, 2012, the unit was shut down to begin a refueling and extended power uprate outage.
REACTOR SAFETY
Cornerstones: Initiating Events, Mitigating Systems, Barrier Integrity
1R04 Equipment Alignment
.1 Partial Equipment Walkdowns
a. Inspection Scope
The inspectors conducted three partial alignment verifications of the safety-related systems listed below. These inspections included reviews using operating procedures and piping and instrumentation drawings, which were compared with observed equipment configurations to verify that the critical portions of the systems were correctly aligned to support operability. The inspectors also verified that the licensee had identified and resolved equipment alignment problems that could cause initiating events or impact the capability of mitigating systems. The inspectors routinely verified that alignment issues were documented in the corrective action program.
- Unit 4 walk down of auxiliary feed water pump C aligned to Train 1 to support maintenance on pump A trip and throttle valve using licensee procedure 4-NOP-075, Auxiliary Feedwater
- Unit 4 walkdown of the residual heat removal pump A aligned for safety injection during maintenance of Pump 4B using licensee procedure 4-OP-050, Residual Heat Removal
- Unit 4 walk down of the Reactor Coolant System level instrumentation during draining of the reactor coolant system using procedure 4-NOP-041.07, Draining the Reactor Coolant System
b. Findings
No findings were identified.
1R05 Fire Protection
.1 Fire Area Walkdowns
a. Inspection Scope
The inspectors toured the following three plant areas to evaluate conditions related to control of transient combustibles, ignition sources, and the material condition and operational status of fire protection systems including fire barriers used to prevent fire damage and propagation. The inspectors reviewed these activities using provisions in the licensee's procedure 0-ADM-016, Fire Protection Plan, and 10 CFR Part 50, Appendix R. The licensee's fire impairment lists were routinely reviewed. In addition, the inspectors reviewed the condition report database to verify that fire protection problems were being identified and appropriately resolved. The inspectors accompanied fire watch roving personnel on a tour of fire protection impairments and risk significant fire areas to assure monitoring of area status and to verify proper identification and handling of transient combustibles. The following areas were inspected:
- Common: Auxiliary Building Breezeway
- Common: Cable Spreading Room
- Common: Control Room
b. Findings
No findings were identified.
1R08 In-service Inspection (ISI) Activities (IP 71111.08P, Unit 4)
a. Inspection Scope
Non-Destructive Examination Activities and Welding Activities
- From November 13-16 and December 10-14 , 2012, the inspectors conducted an on-site review of the implementation of the licensee's In-service Inspection (ISI) Program for monitoring degradation of the reactor coolant system, emergency feed water systems, risk-significant piping and components, and containment systems in Unit 4. The inspectors' activities included a review of non-destructive examinations (NDEs) to evaluate compliance with the applicable edition of the American Society of Mechanical Engineers (ASME) Boiler and Pressure Vessel Code (BPVC),Section XI (Code of record: 2001 Edition with 2003 Addenda, 4 th Interval, 3 rd Period and 1 st Outage), and to verify that indications and defects (if present) were appropriately evaluated in accordance with the requirements of the ASME Code,Section XI, acceptance standards.
The inspectors directly observed and reviewed records for the following NDE mandated by the ASME Code to evaluate compliance with the ASME Code Section XI and Section V requirements and, if any indications and defects were detected, to evaluate if they were dispositioned in accordance with the ASME Code or an NRC-approved alternative requirement.
- Visual Testing (VT):
o Residual Heat Removal (RHR) to Reactor Coolant System (RCS) Loop C Cold Leg Spring Loaded and Constant Weight Hanger, No. SR-499, o RHR to RCS Loop C Cold Leg Double Acting Restraint Hanger, No. 8073-H-810-02, and o Reactor Vessel Bottom Mounted Instrumentation Penetration No. 1, 10, 7, 6, 25, 29, 24, 27, 47, 32, 16 and 42.
- Augmented VT:
o Pressurizer Heater Sleeves, No. 4-PRZ-Heater Sleeves, o High Head Safety Injection (HHSI) Loop A Inside Containment Pipe to Branch Connection, Weld No. 2-SI-1404-10, o HHSI Loop A Inside Containment Pipe to Elbow Connection, Weld No. 2-SI-1404-6, o Chemical Volume Control System (CVCS) to RCS Loop C Hot Leg Elbow to Branch Connection, Weld No. 3-CH-1401-37, and o CVCS to RCS Loop C Hot Leg Pipe to Elbow Connection, Weld No. 3-CH-1401-34.
- Ultrasonic Testing (UT):
o RHR to RCS Loop C Cold Leg Elbow to Pipe Weld No. 10-SI-1403-4
- Augmented UT:
o HHSI Loop A Inside Containment Pipe to Branch Connection, Weld No. 2-SI-1404-10, o HHSI Loop A Inside Containment Pipe to Elbow Connection, Weld No. 2-SI-1404-6, o CVCS to RCS Loop C Hot Leg Elbow to Branch Connection, Weld No. 3-CH-1401-37, and o CVCS to RCS Loop C Hot Leg Pipe to Elbow Connection, Weld No. 3-CH-1401-34.
- Penetrant Testing (PT):
o HHSI Socket to Pipe, Weld No. 2-SI-2406-2 The inspectors reviewed the welding activities referenced below and reviewed associated documents in order to evaluate compliance with procedures and the ASME Code. The inspectors reviewed the following work order, repair and replacement plan, weld data sheets, welding procedures, procedure qualification records, welder performance qualification records, and NDE reports.
- Work Order (WO) No. 40010356-01, Replace 2" line in Boric Acid Solenoid t CVCS Valve 4-368, Class 2, and
- WO 38015275-01, Instrument Air Valve 4-40-336A and Carbon Steel Piping Replacement with Carbon Steel, Class 2, and
- WO 40078181-01, Removal of HHSI Pipe weld defects, Class 2.
During non-destructive surface and volum etric examinations performed since the previous refuelling outage, the licensee did not identify any relevant indications that were analytically evaluated and accepted for continued service. Therefore, no NRC review was completed for this inspection procedure attribute.
PWR Vessel Upper Head Penetration (VUHP) Inspection Activities: For the Unit 4 vessel head, a bare metal visual examination was required this outage pursuant to 10 CFR 50.55a. The inspectors observed portions of the Unit 4 bare metal visual examination and reviewed NDE reports for VUHPs Nos. 7, 19, 28, 33, and 41 to determine if the activities, including the disposition of indications and defects, were conducted in accordance with the requirements of ASME Code Case N-729-1 and 10 CFR 50.55a(g)(6)(ii)(D). In particular, the inspectors evaluated if the required visual examination scope/coverage was achieved and limitations (if applicable) were recorded in accordance with the licensee procedures. Additionally, the inspectors evaluated if the licensee's criteria for visual examination quality and instructions for resolving interference and masking issues were consistent with 10 CFR 50.55a.
The licensee did not identify any relevant indications that were accepted for continued service during the Unit 4 bare metal visual exams. Additionally, the licensee did not perform any welding repairs to the vessel head penetrations since the beginning of the last Unit 4 refueling outage. Therefore, no NRC review was completed for the refueling outage. Therefore, no NRC review was completed for these inspection procedure attributes.
Boric Acid Corrosion Control (BACC) Inspection Activities: The inspectors reviewed the licensee's BACC program activities to ensure implementation with commitments made in response to NRC Generic Letter 88-05, "Boric Acid Corrosion of Carbon Steel Reactor Pressure Boundary," and applicable industry guidance documents. Specifically, the inspectors performed an on-site record review of procedures and the results of the licensee's containment walk-down inspections performed during the current fall refueling outage. The inspectors also interviewed the BACC program owner, conducted an independent walk-down of containment to evaluate compliance with licensee's BACC program requirements, and verified that degraded or non-conforming conditions, such as boric acid leaks, were properly identified and corrected in accordance with the licensee's BACC and corrective action programs.
The inspectors reviewed the following engineering evaluations completed for evidence of boric acid identified in systems containing borated water to determine if degraded
components were documented in the corrective action program. The inspectors also evaluated the following corrective actions for any degraded components to determine if they met the ASME Section XI Code and/or NRC approved alternative.
- AR 01808584 Steam Generator (SG) Tube Inspection Activities: The NRC inspectors observed the following activities and/or reviewed the following documentation and evaluated them against the licensee's technical specifications, commitments made to the NRC, ASME Section XI, and Nuclear Energy Institute (NEI) 97-06 (Steam Generator Program Guidelines):
- Interviewed Eddy Current Testing (ET) data analysts and reviewed 5 samples of ET data.
- Compared the numbers and sizes of SG tube flaws/degradation identified against the licensee's previous outage Operational Assessment.
- Evaluated if the licensee's SG tube ET examination scope included potential areas of tube degradation identified in prior outage SG tube inspections and/or as identified in NRC generic industry operating experience applicable to the licensee's SG tubes.
- Reviewed the licensee's implementation of their extent of condition inspection scope and repairs for new SG tube degradation mechanism(s).
- Reviewed the licensee's repair criteria and processes.
- Verified that Primary-to-secondary leakage (e.g., SG tube leakage) was below three gallons per day, or the detection threshold, during the previous operating cycle.
- Evaluated if the ET equipment and techniques used by the licensee to acquire data from the SG tubes were qualified or validated to detect the known/expected types of SG tube degradation in accordance with Appendix H, Performance Demonstration for Eddy Current Examination, of EPRI Pressurized Water Reactor Steam Generator Examination Guidelines, Revision 7.
- Reviewed the licensee's secondary side SG Foreign Object Search and Removal (FOSAR) activities.
- Reviewed ET personnel qualifications.
Identification and Resolution of Problems: The inspectors performed a review of a sample of ISI-related problems which were identified by the licensee and entered into the corrective action program as condition reports (ARs). The inspectors reviewed the ARs to confirm the licensee had appropriately described the scope of the problem, and had initiated corrective actions. The review also included the licensee's consideration and assessment of operating experience events applicable to the plant. The inspectors
performed this review to ensure compliance with 10CFR Part 50, Appendix B, Criterion XVI, "Corrective Action," requirements. Document reviewed are listed in the Attachment.
b. Findings
No findings were identified.
1R11 Licensed Operator Requalification Program
.1 Resident Inspector Quarterly Review- Annual Requalification Operating Test
a. Inspection Scope
On October 28, 2012, the inspectors assessed licensed operator performance in the plant specific simulator during the annual licensed operator annual requalification operating test. The examination was conducted at the Unit 3 extended power up rate initial conditions. Event simulations were accomplished using Simulator Evaluation PTN 750206900, Loss of Vacuum/Dropped Rod/Loss of 3P09/ATWS. Operators responded to the events using off-normal procedures 3-ONOP-014 for loss of condenser vacuum, 3-ONOP-028.3 for the dropped control rod, and 3-ONOP-003.9 for the loss of the vital instrument panel. Emergency procedures used by the crew to safely mitigate the events included 3-EOP-E-0, Reactor Trip and Safety Injection and 3-EOP-E-2, Faulted Steam Generator Isolation; and 3-EOP-FR-S.1, Response to Nuclear Power Generation/ATWS.
The inspectors specifically checked the simulated emergency classification of Site Area Emergency was done in accordance with licensee procedure, 0-EPIP-20101, Duties of the Emergency Coordinator.
The simulator board configurations were compared with actual plant control board configurations concerning recent power up rate modifications. The inspectors specifically evaluated the following attributes related to operating crew performance and the licensee evaluation:
- Clarity and formality of communication
- Ability to take timely action to safely control the unit
- Prioritization, interpretation, and verification of alarms
- Correct use and implementation of off-normal and emergency operating procedures; and emergency plan implementing procedures
- Control board operation and manipulation, including high-risk operator actions
- Oversight and direction provided by shift supervisor, including ability to identify and implement appropriate TS actions and emergency plan classification and notification
- Crew overall performance and interactions
- Evaluator's control of the scenario and post scenario evaluation of crew performance
b. Findings
No findings were identified.
.2 Control Room Observations
a. Inspection Scope
The inspectors observed the following four focused control room observations and assessed licensed operator performance in the plant and main control room, particularly during periods of heightened activity or risk and where the activities could affect plant safety. These observations routinely included surveillance testing, response to alarms, communications, and coordination of activities. These observations were conducted to verify operator compliance with station operating protocols, such as use of procedures, control and manipulation of components, and communications. On October 30, 2012, the inspectors did a focused observation which included Unit 3 power ascension to the new extended power up rate condition from 87% power to 89% power per 3-GOP-301, Hot Standby to Power Operation. Specifically, the inspectors verified the operators used the Reactivity Maneuver Plan provided by reactor engineering for a one percent an hour power change rate. The inspectors verified that operators borated and moved rods in a controlled manner to meet Technical Specification limits for axial flux deviation. The inspectors observed power ascension from 89% power to 92% power on November 1, 2012, and 92% power to 95% power ascension on November 2, 2012 in the control room for the new extended power up rate conditions at a power rate change of one percent an hour. On November 1, 2012, the inspectors observed operator response to an unexpected lowering of condenser vacuum transient on unit 4 during preparations on the feed water heater drains for the upcoming unit 4 refueling outage activities. The operators entered off normal operating procedure 4-ONOP-014, Loss of Condenser Vacuum, in response to the event.
During these observations, the inspectors focused on the following conduct of operations attributes:
- Operator compliance and use of procedures
- Control board manipulations
- Communication between crew members
- Use and interpretation of plant instruments, indications and alarms
- Use of human error prevention techniques such as peer checks
- Documentation of activities, including initials and sign-offs in procedures
- Supervision of activities, including risk and reactivity management oversight This activity constituted four inspection samples.
b. Findings
Introduction:
A Green self-revealing finding was identified when the licensee failed to follow procedure, 0-ADM-222, Drain and Vent Rig Controls, while installing a temporary drain hose on Turkey Point Unit 4 in-service equipment. Specifically, operations and maintenance workers failed to properly verify a drain line flow path was isolated on the 1B feed water heater prior to removing a valve pipe cap that resulted in an unexpected lowering of condenser vacuum.
Description:
On November 1, 2012, Turkey Point Nuclear Plant Unit 4 experienced an unexpected lowering of condenser vacuum due to the removal of a drain valve pipe cap on the 1B feed water heater. The non-safety related upstream drain isolation valve (4-30-128) was not physically verified to be in its normal closed position as required by safety-related procedure 0-ADM-222, Drain and Vent Rig Controls, prior to removing the pipe cap.
The licensee used procedure 0-ADM-222 as governing guidance to perform both safety and non-safety related plant operations. Unit 4 was in Mode 1, at 100 percent power when the operator at the controls noticed a drop from 762 to 714 megawatts electric (MWe) and a lowering of con denser vacuum from 27.7" mercury (Hg) to 26.0" Hg. The operations work control department had authorized mechanical maintenance to install a drain hose on the in-service 1B feed water heater shell in preparation for the upcoming refueling outage. Instead of physically verifying the position of valve 4-30-128 as required by procedure 0-ADM-222, the licensee relied on their work clearance control computer tracking system to check the position of the valve and incorrectly concluded that the drain valve was closed. As a result, an air in-leakage path was created by mechanical maintenance when the pipe cap downstream of the valve was removed to connect the drain hos e. Off normal operating procedure 4-ONOP-014, Main Condenser Loss of Vacuum, was entered when operators at the controls noticed an unexpected lowering in condenser vacuum. The mechanical maintenance workers immediately notified Operations department they had just installed a drain rig assembly on the feed water heater shell drain valve and coordinated with the operators to close the drain valve which restored vacuum and the plant transient was terminated. The licensee entered this issue into their corrective action program as AR 1819010.
Analysis:
The licensee's failure to verify the closed position of 1B feed water heater drain valve 4-30-128, as required by procedur e 0-ADM-222, prior to removing the pipe cap was a performance deficiency. The inspectors determined the performance deficiency was more than minor using IMC 0612, Appendix B, Issue Screening, because the performance deficiency was associated with the configuration control attribute of the initiating events cornerstone, and adversely affected the cornerstone objective to limit the likelihood of events that upset plant stability and challenge critical safety functions during power operations. Specifically, the failure to verify the position of 4-30-128 resulted in lowering condenser vacuum that could have led to a reactor trip and the unavailability of the main condenser. The inspectors evaluated the finding using the significance determination process for findings at power of IMC 0609, Appendix A, Exhibit 1, Transient Initiators. The inspectors determined the finding was of very low safety significance (Green) because the finding did not result in a reactor trip and a loss of mitigation equipment relied upon to transition the plant to a stable shutdown condition.
The finding was associated with a cross-cutting aspect in the work practices component of the human performance area because the licensee did not define and effectively communicate expectations, or follow the procedural requirement to physically verify valve position during the drain hose installation work. H.4(b) per IMC 0310]
Enforcement:
This finding does not involve enforcement action because no violation of a regulatory requirement was identified. Because this finding did not involve a violation and was of very low safety significance, it is identified as FIN 05000251/2012005-01, Failure to Verify 1B Feed Water Heater Drain Valve Closed.
.3 Annual Review of Licensee Requalification Examination Results
a. Inspection Scope
On November 26, 2012, the licensee completed the annual requalification operating examinations required to be administered to all licensed operators in accordance with 10 CFR 55.59(a)(2). The inspectors performed an in-office review of the overall pass/fail results of the individual operating examinations and the crew simulator operating examinations in accordance with Inspection Procedure (IP) 71111.11, "Licensed Operator Requalification Program." These results were compared to the thresholds established in Inspection Manual Chapter (IMC) 0609, "Significance Determination Process," Appendix I, "Operator Requalification Human Performance Significance Determination Process."
b. Findings
No findings were identified.
1R12 Maintenance Effectiveness
a. Inspection Scope
The inspectors reviewed the following two equipment problems and associated condition reports to verify that the licensee's maintenance efforts met the requirements of 10 CFR 50.65, Requirements for Monitoring the Effectiveness of Maintenance at Nuclear Power Plants, and licensee administrative procedure 0-ADM-728, Maintenance Rule Implementation. The inspectors' efforts focused on maintenance rule scoping, characterization of maintenance problems and failed components, risk significance, determination of a(1) classification, corrective actions, and the appropriateness of established performance goals and monitoring criteria. The inspectors also interviewed responsible engineers and observed some of the corrective maintenance activities. The inspectors verified that equipment problems were being identified and entered into the corrective action program. The inspectors used licensee maintenance rule data base, system health reports, and the corrective action program as sources of information on tracking and resolution of issues.
- Unit 3 CCW system health reports from fourth quarter of 2011 through the second quarter of 2012 were reviewed. The Unit 3 CCW system health was in yellow a(1) status for the fourth quarter of 2011 and first quarter of 2012 for exceeding 3B CCW pump unavailability criteria due to multiple bearing replacements. During the second quarter of 2012, the Unit 3 CCW system health went to white status.
- AR 01793581, 3B Gamma-Metrics wide range channel reliability does not meet performance criteria.
b. Findings
No findings were identified.
1R13 Maintenance Risk Assessments and Emergent Work Control
a. Inspection Scope
The inspectors completed in-office reviews and control room inspections of the licensee's risk assessment of four emergent or planned maintenance activities. The inspectors verified the licensee's risk assessment and risk management activities using the requirements of 10 CFR 50.65(a)(4); the recommendations of Nuclear Management and Resource Council 93-01, Industry Guidelines for Monitoring the Effectiveness of Maintenance at Nuclear Power Plants, Revision 3; and procedures 0-ADM-068, Work Week Management; WM-AA-1000, Work Activity Risk Management; and O-ADM-225, On Line Risk Assessment and Management. The inspectors also reviewed the effectiveness of the licensee's contingency actions to mitigate increased risk resulting from the degraded equipment and the licensee assessment of aggregate risk using FPL procedure OP-AA-104-1007, Online Aggregate Risk. The inspectors evaluated the following risk assessments during the inspection:
- October 25: Unit 3 risk assessment when auxiliary feed water train 2 flow control valves FCV-3-2831 and FCV-3-2832 were removed from service for maintenance, B standby steam generator feed water pump wa s out of service for maintenance, and severe weather threatened the region (Tropical Storm Sandy). The licensee's Green risk characterization was verified using NRC's Standardized Plant Analysis Risk (SPAR) Model for Turkey Point Unit 3 and 4 and risk assessment tool.
- December 5: The performance of the Unit 3 risk assessment was verified and reviewed for accuracy using the licensee risk assessment tool during RCS Flow protection channel tests which requires associated bistables to be tripped. The risk assessment evaluated the aggregate risk. The inspector's observed the use of the tool in the Work Control Center and the Control Room and reviewed the Equipment Out of Service book and Operator Logs to verify the plant configuration. The licensee's Green risk characterization was verified using the NRC's SPAR Model for Turkey Point Unit 3 and 4 and risk assessment tool.
- December 11: Unit 3 risk assessment when 3A ICW/CCW Basket Strainer BS-3-1402 was removed from service for maintenance in conjunction with 4A 4kV bus, 4A emergency diesel generator, and the 4A high head safety injection pump. The licensee's Yellow risk characterizati on was verified using NRC's Standardized Plant Analysis Risk (SPAR) Model for Turkey Point Unit 3 and 4 and risk assessment tool.
- December 13: Unit 3 risk management when the 3A emergency diesel generator fuel oil transfer pump failed to start during its quarterly surveillance test (AR 1832175)
b. Findings
No findings were identified.
1R15 Operability Evaluations
a. Inspection Scope
For the three operability evaluations described in the action requests (AR) listed below, the inspectors evaluated the technical adequacy of licensee evaluations to ensure that TS operability was properly justified and the subject component or system remained available such that no unrecognized increase in risk occurred. The inspectors reviewed the UFSAR to verify that the system or component remained available to perform its intended function. In addition, when applicable, the inspectors reviewed compensatory measures implemented to verify that the plant design basis was being maintained. The inspectors also reviewed a sampling of condition reports to verify that the licensee was identifying and correcting any deficiencies associated with operability evaluations.
- AR 1833717, 3C Intake Cooling Water Pump Tripped During Station Blackout Cross-tie Testing
- AR 1816453, 3B Emergency Diesel Generator Low Lube Oil Evaluation
- AR 1820194, Gas Voiding In U4 Containment
b. Findings
No findings were identified.
1R19 Post Maintenance Testing
a. Inspection Scope
For the five post maintenance tests listed below, the inspectors reviewed the test procedures and either witnessed the testing and/or reviewed test records to determine whether the scope of testing adequately verified that the work performed was correctly completed and demonstrated that the affected equipment was operable. The inspectors used licensee procedure 0-ADM-737, Post Maintenance Testing, in their assessments.
Modifications associated with the extended powerup rate (EPU) are noted.
- Unit 3: 3-OSP-203.2, Train B Engineered Safeguards Integrated Test, sections 7.2 and 7.3 in accordance with engineering change 273225, Emergency Containment Cooler (ECC) Auto-Start Circuit Installation, verifying auto start capability for the swing emergency containment cooler to mitigate a single active failure component
and have two ECC units running (EPU)
- Unit 3: RPS relay replacement and post maintenance testing in accordance with WO 40120591-01 and 3-OSP-049.1, Reactor Protection System Logic Test, after replacement of reactor coolant flow loop B relay RC-4-B, when it was found failed in its de-energized state.
- Unit 3: 3A Train PRB-1-A, power range block permissive relay found de-energized per WO 40195473-01. The post maintenance test was performed in accordance with procedures contained in the referenced work order and 3-OSP-049.1, Reactor Protection System Logic Test, after replacement of the power range block permissive relay PRB-1-A.
- Unit 4: RHR 4B oil sample and motor inspection was conducted per WO 40131754-01 prior to the Unit 4 Cycle 17 Refueling outage. Work was performed using plant procedures 0-GME-005.01, 4.16kV Equipment Grounding and Testing and 0-GMP-102.6, Periodic Collection of Oil Samples from Plant Pumps, Motors, and Other Lubricated Components.
- Common: 0-PME-102.08, MOV Grease Inspection and Stem Lubrication Preventive Maintenance Procedure, performed on AFW Pump C, Trip and Throttle Valve, MOV-6459C, greased and lubricated the throttle valve and ensured proper valve stroke in both the open and close directions, per Work Order 40138214-1.
b. Findings
No findings were identified.
1R20 Unit 4 Refueling and Extended Power Uprate Outage 27 (EPU)
a. Inspection Scope
The inspectors observed selected Unit 4 outage activities starting November 1 to determine whether shutdown safety functions were properly maintained as required by technical specifications and plant procedures. The inspectors evaluated specific performance attributes including operator performance, communications, and risk management. The inspectors reviewed procedures and observed selected activities associated with the outage and conducted walkdowns of systems credited to maintain safety margins and defense in depth. The inspectors verified that activities were performed in accordance with the outage plan, plant procedures, and as appropriate, verified that acceptance criteria were met. Conditions adverse to quality documented by the licensee in the corrective action program were checked daily. Also, management activities were monitored to assure adherence to the outage plan and safe resolution of issues. The inspectors specifically evaluated the following activities:
- New fuel receipt and inspections conducted by the licensee
- Review of the licensee's outage plan and risk management activities prior to the plant shutdown
- Overpressurization Mitigation System testing
- RHR alignment and testing
- Plant shutdown and cool down to Mode 3 with Technical Specification limits.
- Early containment entry and inspection
- Containment hatch closure testing within required time limits.
- Prior to the drain down evolution the NRC inspectors verified the level indication valve alignment inside containment and the removal of the pressurizer safety relief valve to provide for an adequate reactor coolant system vent path.
- Drain down of the reactor coolant system to the reactor vessel flange for removal of reactor head
- Reactor head removal and placement on stand
- Spent Fuel Pool heat exchanger room walk down post core offload.
b. Findings
No findings were identified.
1R22 Surveillance Testing
a. Inspection Scope
The inspectors either reviewed or witnessed the six surveillance tests listed below to verify that the tests met the TS requirements, the UFSAR, and the licensee's procedural requirements and demonstrated that the syst ems were operationally ready to perform their intended safety functions. In addition, the inspectors evaluated the effect of the testing activities on the plant to ensure that conditions were adequately addressed by the licensee staff and that after completion of the testing activities, equipment was returned to the alignment required for the system to perform its safety function. In-service tests (IST) were validated using the licensee's In-service Testing Program, Fourth Ten Year Interval, dated March 11, 2004. The inspectors verified that surveillance issues were documented in the corrective action program. Extended power uprate (EPU) testing was done under NRC Inspection Procedure 71004 guidance.
Containment Isolation Valve Test
- 3-OSP-206.2, Quarterly In-service Valve Testing - Containment Isolation Valve Surveillance Test
- 0-OSP-207.2, Visual Leak Inspection of Systems Outside Containment, Section 7.6.4 Visual Inspection of Unit 4 Volume Control Tank Room
- 0-OSP-005.3, Load Testing of the Station Blackout Cross-Tie
- 4-OSP-050.2A, Residual Heat Removal Train A Test - Standby Alignment
- 3-OSP-075.1, Auxiliary Feedwater Train 1 Operability Verification
- 3-OSP-067.1D, R-3-19 Process Radiation Monitor Test
b. Findings
No findings were identified.
Cornerstone:
Emergency Preparedness 1EP4 Emergency Action Level and Emergency Plan Changes
a. Inspection Scope
The Nuclear Security and Incident Response (NSIR) headquarters staff performed an in-office review of the latest revisions of various Emergency Plan Implementing Procedures (EPIPs) and the Emergency Plan located under ADAMS accession numbers ML12009A082 and ML12184A052, as listed in the Attachment.
The licensee determined that in accordance with 10 CFR 50.54(q), the changes made in the revisions resulted in no reduction in the effectiveness of the Plan, and that the revised Plan continued to meet the requirements of 10 CFR 50.47(b) and Appendix E to 10 CFR Part 50. The NRC review was not documented in a safety evaluation report and did not constitute approval of licensee-generated changes; therefore, these revisions are subject to future inspection. Documents reviewed are listed in the Attachment. This inspection activity satisfied one inspection sample for the emergency action level and emergency plan changes on an annual basis.
b. Findings
No findings were identified.
1EP6 Drill Evaluation
.1 Emergency Preparedness Drill
a. Inspection Scope
On October 25, 2012, the inspectors observed an emergency preparedness drill and the performance of the licensee's emergency response organization. The drill included a simulated Unit 3 MIMS alarm followed by a CVCS letdown radiation monitor R-20 alarm due to fuel cladding damage, requiring an Unusual Event declaration and notification to state of Florida, county officials, and the NRC per 0-EPIP-20101, Duties of the Emergency Coordinator. The scenario progressed to a fire at the intake at 3C ICW pump requiring an Alert notification to the state of Florida and simulated notification to the NRC. The drill scenario progressed to a Site Area Emergency and ended with a General Emergency. The inspectors observed the crew in the plant simulator including simulated implementation of emergency procedures and staff in the Technical Support Center (TSC) using the event classification guidelines and emergency response procedures. During the drill, the inspectors observed the simulator and TSC staff verify that emergency classification and notifications were made in accordance with the licensee emergency plan implementing procedure 0-EPIP-20101. Licensee identified critique items were reviewed and observations were discussed with the licensee to verify that drill issues were identified and captured in the corrective action program.
b. Findings
No findings were identified.
.2 Simulator Based Training Evolution
a. Inspection Scope
On October 15, 2012, the inspectors observed an operating crew in the plant simulator.
The simulation included a steam generator tube leak, a loss of offsite power and a loss of vital AC power in accordance with the licensee's initial/continuing Training Evaluation Scenario 750207603, Loss of Vital AC/Excess RCS Leakage. Plant operators responded to the simulated loss of offsite power with the declaration of an Unusual Event (SU5). With the subsequent failure of one emergency diesel generator, the classification was escalated to an Alert classification (SA5) requiring activation of the emergency response organization. During the drill, the inspectors assessed operator actions to verify that emergency classification and simulated notification to local officials were made in accordance with the emergency plan implementing procedures and 10 CFR 50.72 requirements. The inspectors reviewed the event classifications and notifications to ensure these were made in accordance with licensee procedure, 0-EPIP-20101, Attachments 1 and 2, Turkey Point Classification Tables. Drill critique items were discussed with the licensee and reviewed to verify that drill issues were identified and captured in the licensee's corrective action program.
b. Findings
No findings were identified.
RADIATION SAFETY
Cornerstones: Occupational Radiation Safety (OS) and Public Radiation Safety (PS)
2RS1 Radiological Hazard Assessment and Exposure Controls
a. Inspection Scope
Inspection Planning: The inspectors reviewed licensee Performance Indicator (PI) data for the Occupational Exposure Cornerstone. The inspectors also evaluated the scope of the licensee's internal audit program and reviewed recent assessment results.
Radiological Hazard Assessment: During facility tours, the inspectors directly observed postings and physical controls for radiation area, high radiation area (HRA), and airborne radioactivity locations established within the Unit 4 (U4) containment, Unit 3 (U3) and U4 auxiliary buildings, and radioactive waste (radwaste) processing and storage locations.
The inspectors independently measured radiation dose rates or directly observed conduct of licensee radiation surveys for selected equipment and areas within Radiologically Controlled Area (RCA) locations. Established radiological controls were evaluated for selected U4 Refueling Cycle 27 Outage (U4R27) tasks including reactor sump and steam generator (SG) maintenance activities. The inspectors reviewed and evaluated surveys conducted and records maintained for selected RCA areas and/or refueling outage tasks including surveys for alpha emitters, hot particles, airborne radioactivity, potential dose rate gradients, and upcoming pre-task surveys. The inspectors also discussed changes to plant operations that could contribute to changing radiological conditions since the last inspection.
Instructions to Workers: During facility tours, the inspectors observed and evaluated the adequacy of container labeling and area postings for the previous and current outage activities. For selected outage jobs, the inspectors attended pre-job briefings and reviewed radiation work permit (RWP) details to assess communication of radiological control requirements and current radiological conditions to workers. Electronic Dosimeter (ED) alarm logs were reviewed and workers' responses to dose and dose rate alarms during selected work activities were evaluated. ED alarm set-points and worker stay times were evaluated against radiation survey results.
Contamination and Radioactive Material Control: The inspectors observed surveys of material and personnel being released from the RCA using small article monitor (SAM), personnel contamination monitor, and portal monitor instrumentation. SAM equipment sensitivity, alarm set-points, and release program guidance were discussed with licensee staff. The inspectors also reviewed records of leak tests on selected sealed sources, discussed nationally tracked source transactions with licensee staff, and verified sources within select storage locations. The inspectors also reviewed and discussed with staff processes for release of turbine building components and materials being replaced as part of the ongoing extended power up-rate activities.
Radiological Hazards Control and Work Coverage: Licensee controls for areas where dose rates could change significantly as a result of plant shutdown and refueling operations were reviewed and discussed. The inspectors reviewed RWPs for work within airborne radioactivity areas. For potential HRA tasks involving significant dose rate gradients, e.g., bottom mounted instrumentation maintenance conducted within the reactor sump, the inspectors evaluated the use and placement of whole body and
extremity dosimetry to monitor worker exposure. Controls and their implementation for storage of irradiated material within the U4 spent fuel pool (SFP) were reviewed and discussed with responsible licensee representatives.
Risk-Significant High Radiation Area and Very High Radiation Area Controls
- The inspectors evaluated access barrier effectiveness of Locked High Radiation Area (LHRA) and Very High Radiation Area (VHRA) controls for selected U4 containment building and U3 and 4 reactor auxiliary building (RAB) locations. Procedures for LHRA and VHRA controls were discussed with health physics (HP) supervisors.
Radiation Worker Performance and Radiation Protection Technician Proficiency
- Occupational worker adherence to selected RWPs and Radiation Protection Technician (RPT) proficiency in providing U4 containment and RAB job coverage were evaluated through direct observations and discussions with licensee staff.
Problem Identification and Resolution: Corrective Action Program (CAP) documents associated with radiological hazard assessment and control were reviewed and assessed. The inspectors evaluated the licensee's ability to identify and resolve the issues in accordance with Performance Improvement procedure (PI)-AA-01, Corrective Action Program and Condition Reporting, Revision (Rev.) 3 and PI-AA-204, Condition Identification and Screening Process, Rev. 18. The inspectors also evaluated the scope of the licensee's internal audit program and reviewed recent assessment results.
Radiation protection activities were evaluated against the requirements of Updated Final Safety Analysis Report (UFSAR) Section 11; Technical Specifications (TS) Sections 6.8 Procedures and Programs and 6.12 HRA; 10 CFR Parts 19 and 20; and approved licensee procedures. Licensee programs for monitoring materials and personnel released from the RCA were evaluated against 10 CFR Part 20 and IE Circular 81-07, Control of Radioactively Contaminated Material. Documents reviewed are listed in the
.
The inspectors completed one sample as required by inspection procedure 71124.01.
b. Findings
No findings were identified.
2RS8 Radioactive Solid Waste Processing and Radioactive Material Handling, Storage, and Transportation
a. Inspection Scope
Waste Processing System Program Review: The inspectors reviewed and discussed the status and proposed changes to the radioactive waste processing systems relative to the current Updated Final Safety Analysis Report (UFSAR) and Process Control Program (PCP) documents. The inspectors discussed component function, recent or proposed processing system changes, and radioactive waste (radwaste) program implementation with licensee staff.
For dry active waste (DAW) generated during recent Unit 3 reactor sump and RWST maintenance activities, the inspectors evaluated analyses for hard-to-detect nuclides, reviewed the use of scaling factors, and discussed quality assurance (QA) activities for the waste stream characterizations by the current vendor analysis laboratory. The waste stream sampling methodologies and the resultant data used in select shipping and waste processing activities were evaluated and discussed with responsible radwaste staff.
Radioactive Material Storage
- During walk-downs of radioactive material and radioactive waste storage areas, the inspectors observed the physical condition and labeling of storage containers and the posting of Radioactive Material Areas. The inspectors also reviewed licensee procedural guidance for storage and monitoring of radioactive material. Radiologically Controlled Area (RCA) storage areas evaluated included select Unit 3 and Unit 4 auxiliary building locations, Dry Storage Warehouse, main RCA yard material and waste storage areas, ISFSI facility, and the Radio Tower Road EPU Material Processing area.
Radioactive Waste System Area Walkdowns
- During inspector walk-downs, accessible sections of the liquid and solid radioactive waste (radwaste) processing systems were assessed for material condition and conformance with system design diagrams.
Inspected equipment included radwaste processing and holdup tanks; radwaste system transfer piping, resin and filter components; dewatering system equipment and liquid radioactive waste control panel equipment. In addition, the inspectors reviewed the completion status of selected work order packages associated with liquid waste processing equipment.
Transportation: During the onsite inspection, the inspectors directly observed and evaluated proficiency of the responsible staff during preparation of waste and material shipments. Training provided to radioactive waste staff responsible for preparation of
the shipments to meet Department of Transportation (DOT) regulations was evaluated.
Additional shipping records were reviewed for consistency with licensee procedures and compliance with NRC and DOT regulations. The inspectors reviewed emergency response information, DOT shipping package classification, and waste classification, radiation survey results. Licensee procedures for labeling containers stored onsite were evaluated. In addition, training status for selected individuals currently involved in radioactive material shipping activities was reviewed.
Problem Identification and Resolution: The inspectors reviewed selected Corrective Action Program (CAP) documentation in the areas of radwaste processing and radwaste /radioactive material shipping. The inspectors evaluated the licensee's ability to identify and resolve identified issues in accordance with Performance Improvement procedure (PI)-AA-01, Corrective Action Program and Condition Reporting, Rev. 3, and PI-AA-204, Condition Identification and Screening Process, Rev 18. The inspectors also evaluated the scope of the licensee's internal audit program.
Radwaste processing activities and equipment configuration were reviewed for compliance with the licensee's Process Control Program (PCP), UFSAR Chapter 11; TS 6.8.1, Procedures and Programs, and approved procedures. Waste stream characterization analyses were reviewed against regulations detailed in 10 CFR Part 20, 10 CFR Part 61, and guidance provided in the Branch Technical Position on Waste Classification (1983). Transportation program implementation was reviewed against regulations detailed in 10 CFR Part 20, 10 CFR Part 71, and 49 CFR Parts 172-178.
Training activities were assessed against 49 CFR Part 172 Subpart H. Documents reviewed are listed in the Attachment
The inspectors completed one sample as required by inspection procedure 71124.08.
b. Findings
No findings were identified
OTHER ACTIVITIES
4OA1 Performance Indicator (PI) Verification
a. Inspection Scope
Occupational Radiation Safety Cornerstone: The inspectors reviewed the Occupational Exposure Control Effectiveness PI results for the Occupational Radiation Safety Cornerstone from April 1, 2011, through November 30, 2012. For the assessment period, the inspectors reviewed electronic dosimeter (ED) alarm logs and selected Action Request (AR) / Condition Request (CR) documents related to controls for exposure significant areas and events. The inspectors also reviewed licensee procedural guidance for collecting and documenting PI data. Documents reviewed are listed in the Attachment.
Public Radiation Safety Cornerstone: The inspectors reviewed the Radiological Control Effluent Release Occurrences PI results for the Public Radiation Safety Cornerstone from April 1, 2011, through November 30, 2012. For the assessment period, the inspectors reviewed cumulative and projected doses to the public and ARs related to Radiological Effluent Technical Specifications/Offsite Dose Calculation Manual issues.
The inspectors also reviewed licensee procedural guidance for collecting and documenting PI data. Documents reviewed are listed in the Attachment.
The inspectors completed two of the required samples specified in IP 71151.
b. Findings
No findings were identified
4OA2 Problem Identification and Resolution
.1 Daily Review
a. Inspection Scope
As required by Inspection Procedure 71152, Identification and Resolution of Problems, and to help identify repetitive equipment failures or specific human performance issues for follow-up, the inspectors performed a screening of items entered daily into the licensee's corrective action program. This review was accomplished by reviewing daily summaries of condition reports and by reviewing the licensee's electronic condition report database. Additionally, reactor coolant system unidentified leakage was checked on a daily basis to verify no substantive or unexplained changes.
b. Findings
No findings were identified.
.2 Semiannual Trend Review
a. Inspection Scope
The inspectors performed a review of the licensee's corrective action documents including work request documents, attended shift plant status meetings, and discussed plant operations with the operating staff to identify trends that could indicate the existence of a more significant safety issue. This review was focused on repetitive equipment issues or problems that were not being promptly addressed and corrected. The inspectors review nominally considered the six month period from July 1 to December 31, 2012, but some examples expanded further back in time.
The review also included documents outside the corrective action program, such as system health reports, maintenance rule status reports, daily quality summary reports, the engineering log, surveillance tests, and maintenance lists. The inspectors compared their observations with those in the licensee's trending reports, including station and operations department trending reports.
b. Findings
No findings were identified. The inspectors did not identify any trends not observed by the licensee's trending activities.
4OA3 Event Follow-up
.1 (Closed) Licensee Event Report (L
ER) 50-250/2012-003-00 Condition Prohibited by Technical Specifications Due to Instrument Valve Mispositioning While performing the Unit 3 Main Turbine Valve Alignment in preparation for turbine startup prior to entering Mode 1, operators discovered the turbine pressure transmitters PT-3-446 and PT-3-447 inadvertently isolated. The operator immediately notified the control room and the licensee entered Technical Specifications action statement 3.0.3 because two instrument channels were inoperable. The root isolation valves to the pressure transmitters were found closed and the operators subsequently opened the valves exiting the action statement. It wa s determined that the valves were newly installed and mispositioned during the performance of an Engineering Modification. The root cause analysis documented in AR 1791236 identified a weakness in the Change Request Notice process that failed to identify plant procedure 3-NOP-089, Main Turbine, as an effected document. The licensee took additional actions to correct and prevent this from occurring in the future. The inspector did not identify any performance deficiency and determined that the technical specification non-compliance was of minor significance since it was self-revealing and did not have the potential to lead to a more significant safety concern. The LER is closed.
.2 (Closed) Licensee Event Report (LER) 50-250/2012-004-00 Condition Prohibited by Technical Specifications Due to Instrument Process Line Reversal During Replacement
After increasing power on Unit 3 and entering Mode 1, operators discovered the flow
transmitter 3-FT-476, Channel IV Steam Generator 3A Main Feedwater Flow, was reading lower than expected compared to the other channels. The operator wrote an AR and a work request was issued to troubleshoot the issue. After further evaluation, the channel was declared inoperable and the unit entered Technical Specifications Limiting Condition of Operation 3.3.1,Table 3.3-1, Functional Unit 12 Action 6 which allows continued operation provided the inoperable channel is placed in the tripped condition within 6 hours6.944444e-5 days <br />0.00167 hours <br />9.920635e-6 weeks <br />2.283e-6 months <br />. An investigation by maintenance personnel discovered the high and low sides of the process tubing for the transmitter 3-FT-476 were reversed. The process tubing was repaired and the site exited the action statement and restored the instrument channel. The process tubing for 3-FT-476 was reversed during the recent refueling outage work completed on May 19, 2012. The root cause analysis documented in AR 1800833 identified a weakness in the work instruction and inadequate post maintenance testing. The inspectors documented a self-revealing, non-cited violation (NCV 50-250,251/2012-004-01) of Turkey Point Technical Specification (TS) 3.3.1 Reactor Trip System Instrumentation in Inspection Report 05000250/2012004 and 05000251/20120004. No new findings were identified in the inspector's review of the LER and root cause analysis. The LER is closed.
4OA5 Other Activities
.1 Unit 3 Power Uprate, Inspection Procedure 71004
a. Inspection Scope
The inspectors observed selected plant testing and other power ascension activities during the implementation of the (2350 MWt to 2644 MWt) extended power uprate. The inspectors observed control room and in-plant acvitities during the ascension to the new 100% power level at various plateau levels, and walked down plant systems to ensure adverse conditions were both identified, and if warranted, entered into the corrective action program of resolution.
- Observed power escalation from 235 MWe to 239 MWe over one hour in accordance with licensee procedure 3-GOP-301, Hot Standby to Power Operations
The inspectors also reviewed operator actions, applicable procedure changes, and reviewed selected plant design changes and other inspection activities conducted under the normal baseline inspection program, to ensure an adequate sample of risk-significant attributes required by the governing procedure were evaluated. This included changes to plant emergency operating procedure, as well as associated operator briefings and training to address those actions resulting from a revised steam generator tube rupture analysis.
b. Findings
No findings were identified.
.2 Quarterly Resident Inspector Observations of Security Personnel and Activities
a. Inspection Scope
During the plant inspection period, the inspectors conducted observations of security force personnel and activities to ensure that the activities were consistent with licensee security procedures and regulatory requirements relating to nuclear plant security.
These observations took place during both normal and off-normal plant working hours. These quarterly resident inspector observations of security force personnel and activities did not constitute any additional inspection samples. Rather, they were considered an integral part of the inspection activities.
b. Findings
No findings were identified.
.3 (Discussed) Temporary Instruction (TI) 2515/182 - Review of the Implementation of the Industry Initiative to Control Degradation of Underground Piping and Tanks, Phase 1
a. Inspection Scope
Leakage from buried and underground pipes has resulted in ground water contamination
incidents with associated heightened NRC and public interest. The industry issued a guidance document, Nuclear Energy Institute (NEI) 09-14, "Guideline for the Management of Buried Piping Integrity," (ADAMS Accession No. ML1030901420), to describe the goals and required actions (commitments made by the licensee) resulting from this underground piping and tank initiative. On December 31, 2010, NEI issued Revision 1 to NEI 09-14, "Guidance for the Management of Underground Piping and Tank Integrity," (ADAMS Accession No. ML110700122), with an expanded scope of components which included underground piping that was not in direct contact with the soil and underground tanks. On November 17, 2011, the NRC issued TI-2515/182 "Review of the Industry Initiative to Control Degradation of Underground Piping and Tanks," to gather information related to the industry's implementation of this initiative.
The inspectors reviewed the licensee's programs for buried pipe and underground piping and tanks in accordance with TI-2515/182 to determine if the program attributes and completion dates identified in Sections 3.3 A and 3.3 B of NEI 09-14, Revision 1 were contained in the licensee's program and implementing procedures. For the buried pipe and underground piping program attributes, with completion dates that had passed, the inspectors reviewed records to determine if the attribute was in fact complete and to determine if the attribute was accomplished in a manner which reflected good or poor practices in program management.
b. Observations and Findings
The licensee's buried piping and underground piping and tanks program was inspected in accordance with paragraphs 03.01.a through 03.01.c of TI-2515/182 and was found to meet all applicable aspects of NEI 09-14 Revision 1, as set forth in Table 1 of the TI.
Based upon the scope of the review described above, Phase I of TI-2515/182 was complete. No findings were identified.
.4 (Closed) Temporary Instruction 2515/188 - Inspection of Near-Term Task Force Recommendation 2.3 Seismic Walkdowns
a. Inspection Scope
From September 18-19, 2012, the inspectors independently performed their walkdown of the Unit 3 Battery Rack Room and the 4160V Switchgear Room and verified that the licensee confirmed that the following seismic features associated with the 3B Battery Rack, Sequencer 3C23A-Cabinet, and the Switchgear Room 3B-Air Handling Unit, were free of potential adverse seismic conditions:
- Anchorage was free of bent, broken, missing or loose hardware
- Anchorage was free of corrosion that is more than mild surface oxidation
- Anchorage was free of visible cracks in the concrete near the anchors
- Anchorage configuration was consistent with plant documentation
- SSCs will not be damaged from impact by nearby equipment or structures.
- Overhead equipment, distribution systems, ceiling tiles and lighting, and masonry block walls are secure and not likely to collapse onto the equipment
- Attached lines have adequate flexibility to avoid damage
- The area appears to be free of potentially adverse seismic interactions that could cause flooding or spray in the area
- The area appears to be free of potentially adverse seismic interactions that could cause a fire in the area
- The area appears to be free of potentially adverse seismic interactions associated with housekeeping practices, storage of portable equipment, and temporary installations (e.g., scaffolding, lead shielding)
Additionally, inspectors verified that items that could allow the spent fuel pool to drain down rapidly were added to the Seismic Walkdown Equipment List (SWEL) and these items were walked down by the licensee.
b. Observations and Findings
Observations made during the walkdown that could not be determined to be acceptable were entered into the licensee's corrective action program for evaluation. For example, some electrical cabinets associated with items on the SWEL could not be opened due to protected train requirements. It is the licensee's intention to inspect those items at the first opportune time (most likely the next outage for each respective unit). No findings were identified.
.5 Independent Spent Fuel Storage Installation (ISFSI) Walkdown (IP 60855.1)
a. Inspection Scope
On October 10, 2012, the inspectors toured the independent spent fuel storage installation and observed plant operators perform their daily walk down using the listed procedure. The inspectors observed each cask building temperature indicator and passive ventilation system to be free of any obstruction thus allowing natural draft convection decay heat removal through the air inlet and air outlet openings. The inspectors observed associated cask building structures to be structurally intact and security access controls to the ISFSI area to be functional.
- 0-OSP-200.5, Miscellaneous Test, Checks, and Operating Evolutions.
b. Findings
No findings were identified.
4OA6 Meetings, Including Exit
Exit Meeting Summary
The resident inspectors presented the inspection results to Mr. Kiley and other members of licensee management on January 16, 2013. The inspectors asked the licensee whether any of the material examined during the inspection should be considered proprietary information. The licensee did not identify any proprietary information.
ATTACHMENT: SUPPPL EMENTAL INFORMATION
SUPPLEMENTAL INFORMATION
KEY POINTS OF CONTACT
Licensee personnel
- G. Alexander, FPL Engineering
- C. Cashwell, Radiation Protection Manager
- M. Crosby, Quality Manager
- P. Czaya, Licensing
- M. Epstein, Emergency Preparedness Manager
- A. Figueroa, Design Engineer
- J. Garcia, Engineering Manager
- M. Jones, Operations Manager
- M. Kiley, Site Vice-President
- E. Korkowski, SG Program Manager
- E. Lyons, Welding/Repair Replacement
- G. Melin, Assistant Operations Manager
- G. Mendoza, Chemistry Manager
- E. McCartney, Plant General Manager
- S. Mihalakea, Licensing
- J. Pallin, Maintenance Manager
- J. Patterson, Fire Protection Supervisor
- K. Remington, Engineering
- D. Sluzka, Work Controls Manager
- P. Tienmann, Licensing
- R. Tomonto, Licensing Manager
NRC
- S. Stewart, Senior Resident Inspector
- M. Barillas, Resident Inspector
ITEMS OPENED, CLOSED, AND DISCUSSED
Opened and Closed
- 05000251, 2012005-01 FIN Failure to Verify 1B Feedwater Heater Drain Valve Closed (Section 1R11.2)
Closed
- 05000250, 251/2515/188 TI Inspection of Near-Term Task Force Recommendation 2.3 Seismic Walkdowns (Section
- 4OA5.4)
- Attachment
- 05000250/LER-2012-003-00 LER Condition Prohibited by Technical Specifications Due to Instrument Valve Mispositioning (Section
- 4OA3.1)
- 05000250/LER-2012-004-00 LER Condition Prohibited by Technical Specifications Due to Instrument Process Line Reversal During
- Replacement (Section 4OA3.2)
Discussed
- 05000250, 251/2515/182 TI Temporary Instruction (TI) -2515/182 - Review of the Implementation of the Industry Initiative to Control Degradation of Underground Piping and Tanks, Phase 1 (Section 4OA5.3)
LIST OF DOCUMENTS REVIEWED
Section 1R08: Inservice Inspection (ISI) Activities
- Corrective Action
- AR 2008-14563
Procedures
- Areva Document # 03-1246524, Instructions for Plug Inspection, Rev. 11
- Areva Document # 51-5029214-10 Qualified Eddy Current Techniques for Turkey Point (PTN)
- Units 3 & 4 Areva Examination Technique Specification Sheet 1 for
- PTN4-EOC26 Rev. 0
- Areva Examination Technique Specification Sheet 2 for
- PTN4-EOC26 Rev. 0
- Areva Examination Technique Specification Sheet 3 for
- PTN4-EOC26 Rev. 0
- Areva Examination Technique Specification Sheet 4 for
- PTN4-EOC26 Rev. 0
- NDE 3.3, Liquid Penetrant Examination Solvent Removable, Visible Dye Technique, Rev. 13 NDE 3.5, Liquid Penetrant Examination in Accordance with Construction Codes, Rev. 4 NDE 4.15, Visual Examination ASME Section XI Code Case N-722-1 and N-729-1, Rev. 3
- NDE 4.2, Visual Examination
- VT-2 Conducted During System Pressure Test, Rev. 10
- Attachment NDE 4.3, Visual Examination
- VT-3, Rev. 11 NDE 5.31, Ultrasonic Examination Technique for Thermal Fatigue Cracking in Piping
- 1.5" to
Drawings
- ISI-002, UT Calibration Block Piping 18" Diameter, Rev. 6
- UT-44, 3"-SS Pipe Standard, No.
- HT-2P3278, Rev. 0
Other Documents
- 0-ADM-537, Boric Acid Corrosion Control Program, Rev. 6 Areva Document # 03-9195093, Florida Power and Light Turkey Point Unit 4 Secondary Side Inspection On-Site Report, Rev. 0 Areva Personnel Certification, D. Austin Areva Personnel Certification, G. Chapman Areva Personnel Certification, T. Allen Bonney Forge CMTR No.
- 311480, Heat No. 44027
- Boric Acid Corrosion Control Program Quick Ho
t Self Assessment Plan and Report, 8/1-30/2011 Curtis Wright Personnel Certification, J. Timm Curtis Wright Personnel Certification, K. Nelson Curtis Wright Personnel Certification, T. Moore General Electric UT Probe Certificate of Conformity, S/N SI0071
- Ladish Valves CMTR No.
- 1003598 Lambert Macgill Thomas Personnel Certification, B. Kissack Lambert Macgill Thomas Personnel Certification, J. Fuller Lambert Macgill Thomas Personnel Certification, M. Shoemaker Magnaflux Dual Purpose Penetrant Batch No.
- 965028 Certification Magnaflux Spotcheck Developer Batch No. 08F02K, 08M01K Certification Panametrics/Epoch 4 UT Instrument Linearity Record, S/N
- 081574301
- PTN-ENG-SESJ-10-052, Condition Monitoring and Operational Assessment for the Turkey Point Unit 4 Steam Generators Based on Eddy Current Examination End of Cycle 24, November 2009, Rev. 0
- PTN-ENG-SESJ-102-096, Degradation Assessment for Turkey Point Unit 3 and 4 Steam Generators, Update for the Turkey Point Unit 4 End-of-Cycle 25 Refueling Outage, Rev. 0
- PTN-ENG-SESJ-12-029, Degradation Assessment for Turkey Point Unit 3 and 4 Steam Generators, Update for the Turkey Point Unit 4 End-of-Cycle 26 Refueling Outage, Rev. 01 Sandvik Certified Materials Test Report (CMTR) No. A/09-859488, Heat No.
- 521700, Stainless Steel Temperature Indicator Calibration Form, Serial No.
- 263086
- Ultragel Certified Test Report, Batch No. 07125
- UT Calibration Standard Mill Test Report, No. J2009
- Attachment
Section 1EP4: Emergency Action Level and Emergency Plan Changes
- Change Packages Radiological Emergency Plan, Revisions 54 and 55
- 0-EPIP-20126, "Off-site Dose Calculations," Revision 1
- 0-EPIP-20132, "Technical Support Center (TSC) Activation and Operation," Revision 2A
- 0-EPIP-20133, "Operations Support Center (OSC) Activation and Operation," Revision 1
- 0-EPIP-20101, "Duties of Emergency Coordinator," Revision 6
- Section 2RS01:
- Radiological Hazard Assessment and Exposure Controls
Procedures
and Guidance Documents
- 0-ADM-023, Inventory Control and Accounting of Radioactive Sources, Rev. 2
- 0-HPA-001, Radiation Work Permit Initiation and Termination, Rev. 3
- 0-ADM-600, Radiation Protection Manual, Rev. 1
- 0-ADM-605, Control of Radioactive Material, Rev. 1
- 0-HPA-031.2, Multibadge Exposure Monitoring, 0A
- 0-HPS-021.3, Identification, Survey, and Release of Material for Unrestricted Use, Rev. 4
- RP-AA-100-1001, Radiation Protection Conduct of Operations Guideline, Rev. 1
- RP-AA-101-2004, Method for Monitoring and Assigning Effective Dose Equivalent (EDE) for High Dose Gradient Work, Rev. 2
- RP-SR-101-1003, Personnel Contamination Monitoring and Decontamination, Rev. 3
- RP-SR-102-1001, Area Radiological Surveys and Analysis, Rev. 2
- RP-SR-103-1001, Posting Requirements for Radiological Hazards, Rev. 5
- RP-SR-103-1002, High Radiation Area Controls, Rev. 3
- RP-TP-101-1000, Exposure Investigations, Rev. 0A
- RP-TP-103-1003, RP Survey Requirements for Extended Power Uprate Secondary Side
- Components and Material, Rev. 0A
- RP-TP-107-1001, Storage of Highly Radioactive Material in the Reactor Cavity or Spent Fuel
- Pool, Rev. 0
- Records and Data Reviewed Quick Hit Self-Assessment, "Crud Burst Control Self Assessment," 02/24/12
- Turkey Point Nuclear Oversight Report,
- PTN-12-002-Radiation Protection and Radwaste Audit,
- 03/15/12
- Quick Hit Self-Assessment, Inadequate Collective Radiation Exposure Performance
- Improvements, Ammended 11/18/11 Focused Self Assessment #01715112, Alpha Monitoring Program, dated 05/25/12
- 2012 NSTS Annual Inventory Reconciliation, Dated 01/18/12
- Radioactive Source Leak Test Results, Dated 10/26/12
- U3 Spent Fuel Pool Status of Cells with Trash Baskets and With Loose Trash, Dated 11/27/12
- HP 14.14. HP Radioactive Source Inventory Report, Dated 11/15/12 U4R27 Outage Radiation Protection Shift Turnover, dated 12/11/12
- Lesson Plan,
- PTN 2402904, "Pre-Outage Training for RP Personnel." Dated 09/26/12
- Air Calculation Sheet, (ACS) A/S Log Ref No. P0-12-6331, U4 RCB 'A' S/G Platform, Dated
- 2/09/12
- ACS, A/S Log Ref No. P0-12-6375, U4 RCB 'A' S/G Platform, Dated 12/10/12 ACS, A/S Log Ref No. P0-12-6453, U4 RCB 'A' S/G Platform, Dated 12/11/12 ACS, A/S Log Ref No. P0-12-6330, U4 RCB 'B' S/G Platform, Dated 12/09/12
- ACS, A/S Log Ref No. P0-12-6384, U4 RCB 'B' S/G Platform, Dated 12/10/12
- Attachment ACS, A/S Log Ref No. P0-12-6455, U4 RCB 'B' S/G Platform, Dated 12/11/12 ACS, A/S Log Ref No. P0-12-6333, U4 RCB 'C' S/G Platform, Dated 12/09/12 ACS, A/S Log Ref No. P0-12-6457, U4 RCB 'C' S/G Platform, Dated 12/11/12
- ACS, A/S Log Ref No. P0-12-6445, U4 RCB Rx Sump Flow Level Test, Dated 12/11/12
- ACS, A/S Log Ref No. P0-12-6550, U4 RCB Rx Sump Outside, Dated 12/12/12
- ACS, A/S Log Ref No. P0-12-6517, U4 RCB Rx Sump General Area, Dated 12/12/12
- HP-44:76, Survey Log No. 12-12406, Unit-4
'A' Steam Generator, Dated 12/04/12
- HP-44:76, Survey Log No. 12-12420, Unit-4 'C' Steam Generator, Dated 12/04/12
- HP-47:48, Survey Log No. 12-12917, Unit-4 'C' Steam Generator, Dated 12/11/12
- HP-47:48, Survey Log No. 12-12923, Unit-4 'C' Steam Generator, Dated 12/12/12
- HP-44:65, Survey Log No. 12-10831, Unit 4 Reactor Sump Initial Survey, Dated 11/07/12
- HP-44:65, Survey Log No. 12-10958, Unit 4 Reactor Sump Insulation Survey, Dated 11/09/12
- HP-44:65, Survey Log No. 12-12843, Unit 4 Reactor Sump Survey, Dated 12/10/12
- HP-44:65, Survey Log No. 12-12968, Unit 4 Reactor Sump Survey, Dated 12/12/12
- HP-21, Dose Rate Alarm Check-List, AR#01831518, Dated 12-10-12
- HP-108.1, EDE Multibadge Data Sheet, dated 12/12/12
- HRA Briefing and Entry Log, dated 12/12/12
- RP-TP-103-1002-F10, "High Radiation Area Controls," LHRA Key Inventory Form, undated RP Shift HRA/LHRA/VHRA Restricted Key Inventory Logs, Dated 12/13/12
- RWP No. 12-4002, Radiation Protection Outage Containment Activities, Rev 3
- RWP No. 12-4024, Bottom Mounted Instrumentation Project (BMI), Rev. 3
- RWP No. 12-4102, U4R27 Thimble Tube Replacement Work on 58', Rev 2 RWP No. 12-4205, Outage Locked High Radiation Area Work, Rev 3 SEN0016A- RWP and Task Descriptions, Dated 11/19/12
- Corrective Action Program (CAP) Documents
Action Request
(AR)
- 1702878, Alpha Contamination Issues
- AR 01824368, Review of TLD Separations
- AR 01664707, Site Dose Delta Between Estimate and Actual
- AR 01696554, Recovery Plan For Increased Dose Rates From U3 Crud Burst
- AR 01668099, U3 SFP Handling Tool Found Unlocked
- AR 01745321, RP Technician not Meeting Dosimetry Use Expectations
- AR 01689935, Unauthorized Issuance of Radioactive Sources W/O RP Escort
- AR 01774679, RWP Radiation Setpoints Very High
- AR 01712443, Radiation Area Boundary Greater Than 5 Mr/Hr Section 2RS08:
- Radioactive Solid Waste Processing and Radioactive Material Handling, Storage, and Transportation
Procedures
and Guidance Documents
- Administrative Procedure (ADM)-605, Control of Radioactive Material, Revision (Rev.) 1
- Florida Power & Light, Turkey Point Nuclear Station Nuclear Training Department, Lesson Package Number (No.)
- 2400080,Radioactive Material Shipping, 08/31/11 0-HPA-045, Process Control Program, Rev. 0
- RP-AA-108-1002, Shipment of Radioactive Material, Rev. 1
- RP-AA-108-1003, Radioactive Materials Surveys for Shipment, Rev. 1
- Attachment
- RP-AA-108-1004, Packaging Radioactive Materials for Shipment, Rev. 0 0-NCOP-501,
- DTS-WPS Media Sluice, Rev. 1 0-NCOP-502, DTS Media Dewatering, 5/20/10
- 0-HPS-040.5, 10 CFR61 Compliance and Radioactive Waste/Material Shipment Classification and Characterization, 06/22/10
- Records and Data Reviewed Radioactive Waste Manifest Tracking Log, Calendar Year (CY) 2011 and Year-to-Date (YTD)
- 2012
- Radioactive Material Shipment Tracking Log, Calendar Year (CY) 2011 and Year-to-Date (YTD)
- 2012
- Radioactive Material Shipment (M)-12-149, UN3321, Radioactive material, low specific activity(LSA-II), 7 Fissile Excepted, 1 Metal Box UniTech Used Material 40' SeaLand Container, 12/12/12
- Radioactive Waste Shipment, (W)-12-043, UN3321, Radioactive material, low specific activity(LSA-II), 7 Fissile Excepted, 2 Metal Boxes 2012, Dry Active Waste (DAW), 12/12/12
- Radioactive Waste Shipment, W-12-029, UN3321, Radioactive material, low specific activity (LSA-II), 7 Fissile Excepted, 2 Metal Boxes, 2012 DAW, 07/26/12 Radioactive Waste Shipment, W-12-028, UN3321, Radioactive material, low specific activity(LSA-II), 7 Fissile Excepted, 1 Metal Box, 2012 DAW, 1 Metal Box
- RWST-Sump DAW,
- 07/24/12
- Radioactive Waste Shipment, W-12-026, UN3321, Radioactive material, low specific activity(LSA-II), 7 Fissile Excepted, 12 Metal Boxes, DAW in 20 foot (') Sealand Container
- 07/12/12 Radioactive Material Shipment, M-12-091, UN3321, Radioactive material, low specific activity(LSA-II), 7 Fissile Excepted, 1 Metal Box AREVA
- 9011352, 06/28/12
- Radioactive Material Shipment, M-12-069, UN3321, Radioactive material, low specific activity(LSA-II), 7 Fissile Excepted, 1 Metal Box UniTech Used Material, 40' SeaLand Container, 05/26/12 Radioactive Material Shipment, M-12-006, UN3321, Radioactive material, low specific activity(LSA-II), 7 Fissile Excepted, 1 Metal Box, Spent Fuel Pool Handling Tool, 02/17/12
- CFR Part 61 Analysis for 2012 Dry Active Waste (DAW), 07/16/2012
- 94010128, 3B RCDT pump keeps tripping off
- WR 400059695, Annunciator did not flash while testing alarm panel
- WR 94059695, Control switch for
- CV-3-4658A will not go to close
- LCV-4-1003B limit switch shows closed when valve is open
- Corrective Action Program (CAP) Documents Turkey Point Nuclear Oversight Report No.
- PTN-12-002, Radiological Protection and Radwaste,
- 03/15/2012
- AR 01790284, Eight pieces of M&TE were disposed of as radwaste
- AR 01809883, Waste class not marked on container in accordance with disposal facility waste acceptance criteria
- AR 01748532, Replace secondary liner in radwaste skid
- AR 01772330, Radioactive shipment egress prevented by west end of NAB
- AR 01770861, RWST waste seal and will require additional handling prior to shipment Attachment
- AR 01715311, Informational radiological posting not removed from non-radiologically contaminated equipment
- AR 01700085, Delay in receipt of radioactive material shipment,
- AR 1747168, Initial Cavity survey After Draining
- AR 1760652, Locked High Radiation Area Not Secured Properly
- AR 1823307, Boilermaker Moved Locked HRA Sign
- AR 1788351, Inadequate HRA Postings
- AR 1752780, Individual Did Not Acknowledge Dose Rate Alarm on Sentinel
Procedures
and Guidance Documents
- 0-ADM-032, NRC Performance Indicators Turkey Point, Rev. 4
- Records and Data Reviewed Annual Radioactive Effluent Release Report, January 2011 through December 2011
- AR 01643894, Documentation of unplanned release
- AR 01687974, Inability to close liquid release L-2011-111 B-MT
- Annual Radioactive Effluent Release Report Gaseous Effluent, Site Ground Releases, as of December 12, 2012 0-NCOP-006, Gas Gamma Beta Dose Summary Sheet, December 2011
- 0-NCOP-006, Liquid Dose Summary Sheet, December 2011
- 0-NCOP-006, Gas Gamma Beta Dose Summary Sheet, November 2012
- 0-NCOP-006, Liquid Dose Summary Sheet, November 2012
- PTN Quarterly PI Reports, Dated 2
nd Qtr 2011 to September 2012 List of Dose and Dose Rate alarms for the periods 04/02/11 - 11/20/12 Exposure Investigation Reports, dated from 04/01/11 through 12/12/12
- Section 4OA5.1:
Procedures
- ER-AA-102, Buried Piping Program, Rev. 1
- ER-AA-102-1000, Buried Piping Examination Procedure, Rev. 01
- Corrective Action Documents
Other Documents
- Buried Piping Program Health Report, 1 Quarter 2011 Buried Piping Program Health Report, 1 Quarter 2012
- Buried Piping Program Health Report, 2 Quarter 2011
- Buried Piping Program Health Report, 2 Quarter 2012
- Buried Piping Program Health Report, 3 Quarter 2011
- Buried Piping Program Health Report, 3 Quarter 2012 Buried Piping Program Health Report, 4 Quarter 2011
- NEI 09-14 Prioritization of Underground Piping, June 2012
- Attachment Quick Hit Self Assessment Report, 2011 Fleet Buried Piping Program Self-Assessment, 10/3/2011
- Quick Hit Self Assessment Report, QHSA for NRC Buried Piping Inspection
- TI-182, September
- 14-19, 2012 Report No.
- 1016456, Recommendation for an Effective Program to Control Degradation of Buried Piping, December 2008 Schedule for Buried and Underground Piping Examinations Turkey Point Buried Piping Program Basis Document, Revision 0 Turkey Point Power Station Underground Piping and Tanks Examination Plan, Rev. 0
- Unit 3 Circulating Water Pipe NDE Inspection, August 2012
- Section 4OA5.4:
- 1025286 "Seismic Walkdown Guidance for Resolution of Fukushima Near-Term Task Force Recommendation 2.3 Turkey Point Seismic Walkdown Equipment List (SWEL) 1 and 2
- Various Seismic Evaluation Training Course Certifications Area Walk-By Checklist and Seismic Walkdown Checklist for Areas 347 and 368