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{{#Wiki_filter://g(c~ROBERTC. | {{#Wiki_filter://g(c~ROBERTC.MECREDYVicePresident NvcfeorOperotions ROCHESTER GASANDELECTRICCORPORATION | ||
~89EASTAVENUE ROCHESTER N.Y.Id6d9.0MI AREACODE71654'6-2700 January15,1998U.S.NuclearRegulatory Commission DocumentControlDeskAttn:GuyS.VissingProjectDirectorate I-1Washington, D.C.20555 | |||
==Subject:== | ==Subject:== | ||
| Line 23: | Line 24: | ||
==DearMr.Vissing:== | ==DearMr.Vissing:== | ||
Inaccordance with10CFRPart21,Reporting ofDefectsandNoncompliance, Section21(d)(3)(ii),whichrequires"Writtennotification totheNRC...ontheidentificatiohi ofadefectorafailuretocomply",theattached10CFR21reportisherebysubmitted. | |||
10CFR2130DAYWRITTENREPORTPage2I.' | Verytrulyyours,RobertC.Mecredxc:Mr.GuyS.Vissing(MailStop14B2)ProjectDirectorate I-1DivisionofReactorProjects-I/IIOfficeofNuclearReactorRegulation U.S.NuclearRegulatory Commission Washington, D.C.20555RegionalAdministrator, RegionIU.S.NuclearRegulatory Commission 475Allendale RoadKingofPrussia,PA194066IU.S.NRCGinnaSeniorResidentInspector | ||
'tt80i2203b5 | |||
'sI80ii5PDRADQCK05000244SPDRIIIIIII/IIIIIIIIIlIIIIIIIIIIIIIIIIIIIII h~. | |||
10CFR2130DAYWRITTENREPORTPage2I.'AMEANDADDRESSOFTHEINDIVIDUAL INFORMING THECOMMISSION: | |||
NAME:RobertC.Mecredy'icePresident NuclearOperations GroupADDRESS:Rochester Gas&ElectricCorporation 89.EastAvenueRochester, NewYork14649'IDENTIFICATION OFTHEFACILITY, THEACTIVITY, ORTHEBASICCOMPONENT SUPPLIEDFORSUCHFACILITYWHICHFAILSTOCOMPLYORCONTAINSADEFECT:IThefacilityistheR.E.GinnaNuclearPowerPlant.Thebasiccomponent istheshunttripassemblyonthe"B"Emergency DieselGenerator (EDG)SupplyBreakertoBus16.ThisbreakerisaWestinghouse DB-75aircircuitbreakerandtheGinnaequipment identification numberisEIN52/EG1B1, Theshunttripassemblywasinstalled onthisbreakerinMay,1995,usingsparepartspurchased in1977.IDENTIFICATION OFTHEFIRMCONSTRUCTING THEFACILITYORSUPPLYING THEBASICCOMPONENT WHICHFAILSTOCOMPLYORCONTAINSADEFECT:Theshunttripassemblywassuppliedby:Westinghouse ElectricCorporation PowerSystemsSwitchgear Division700BraddockAvenueEastPittsburgh, PA15112NATUREOFTHEDEFECTORFAILURETOCOMPLYANDTHESAFETYHAZARDWHICHISCREATEDORCOULDBECREATEDBYSUCHDEFECTORFAILURETOCOMPLY:Theshunttripcoilplungerispartoftheshunttripandalarmswitchassembly. | |||
Theplungeroftheshunttripassemblywasbindingintheshunttripcoil.Whenactivated, thebreaker's shunttripcoilplungerpullsthebreakertripperbartotripthebreaker.Theboundplungerwasnotreturning toitsdeenergized position. | |||
Thebreakertripperbarwasbeingmaintained inthetripfreeposition, preventing theDB-75aircircuitbreakerfromclosing. | |||
r't,I/ | r't,I/ | ||
Page3Testingofthe"B" | Page3Testingofthe"B"EDGSupplyBreakertoBus16wasperformed inNovember, 1997,duringthe1997outage.'Duringthistesting,thebreakerfailedtoclose.Thebreakercouldnotbeclosedelectrically ormanually, becausetheshunttripcoilplungerwasmaintaining thetripperbarinthetripfreeposition. | ||
Thisfailurewouldpreventthe"B"EDGfromsupplying powertothesafeguards loadsonBus16.Thisisconsidered amajordegradation since,inconjunction withasinglefailureontheredundant train,requiredsafetyfunctions couldnotbeperformed. | |||
~f) | THEDATEONWHICHTHEINFORMATION OFSUCHDEFECTORFAILURETOCOMPLYWASOBTAINED: | ||
Theinformation wasobtainedduringtestingperformed onNovember14,1997.INTHECASEOFABASICCOMPONENT WHICHCONTAINSADEFECTORFAILSTOCOMPLY,THENUMBERANDLOCATIONOFALLSUCHCOMPONENTS INUSEAT,SUPPLIEDFOR,ORBEINGSUPPLIEDFORGINNASTATION:TherearesixWestinghouse DB-75breakerspermanently installed atGinnaStation,insafeguards buses14,and16.Oneofthesebreakersismanuallyoperatedandtheshunttripcoilisnotused.Inaddition, thereisonespareDB-75breakerinstock.Withtheexception ofthe52/EG1B1breaker,thesebreakersstillhavetheiroriginalshunttripassemblies installed. | |||
The52/EG181breakeristheonlyDB-75breakerthathashadtheshunttripassemblyreplaced. | |||
Thereplacement shunttripassemblythatfailedwasoneoftenpurchased in1977asspares.THECORRECTIVE ACTIONWHICHHASBEEN,ISBEING,ORWILLBETAKEN;THENAMEOFTHEINDIVIDUAL ORORGANIZATION RESPONSIBLE FORTHEACTION;ANDTHELENGTHOFTIMETHATHASBEENORWILLBETAKENTOCOMPLETETHEACTION:Corrective actioniscomplete. | |||
Thefailedshunttripassemblywasreplacedwithasparefromstock.Theassemblywasmanuallyandelectrically bench'tested priortobeingreturnedtooperablestatus.Theremaining eightassemblies instockwereinspected. | |||
Twoassemblies hadcoilplungersthatdidnotfullyreturntothedeenergized positionduringmanualmanipulation. | |||
Thesewereremovedfromstock.1TheotherDB-75breakerswerevisuallyinspected. | |||
Acceptable plungermovementisindicated byadequateplungertotripperbargapandfullretraction ofthealarmswitchattachment pushrod.Noadditional bindingconcernswerefound. | |||
Page4TheProcurement AnalysisForm(PAF)fortheshunttripassemblywasappended. | |||
Priortoreordering, thePAFnowrequirestheadditionofplungermovementverification totheassemblyacceptance plan.Westinghouse wascontacted. | |||
Therehavebeennootherreportedeventsofthisnature'that Westinghouse isawareof.Acheckofindustryoperational eventsdidnotidentifysimilarbreakerfailure.ANYADVICERELATEDTOTHEDEFECTORFAILURETOCOMPLYABOUTTHEFACILITY, | |||
: ACTIVITY, ORBASICCOMPONENT THATHASBEEN,ISBEING,ORWILLBEGIVENTOPURCHASERS ORLICENSEES: | |||
Receiptinspection couldverifyacceptable plungermovement. | |||
DuringDB-75breakermaintenance, considerverifying thattheshunttripcoilplungermovesfreely.inthecoilbyverifying adequateplungertotripperbargapandfullretraction ofthealarmswitchattachment pushrod. | |||
~f)JGENERALINFORMATION orOTHEREVENTNUMBER:33442LICENSEE: | |||
ROCHESTER GASRELECTRICCORPCITY:ROCHESTER REGION:1COUNTY:STATE:NYLICENSES: | |||
AGREEMENT: | |||
YDOCKET:NOTIFICATXON DATE:12/22/97NOTIFICATION TIME:09:10[ET]EVENTDATE:11/14/97EVENTTIME:12:00[EST] | |||
LASTUPDATEDATE:12/22/97NOTIFICATIONS NRCNOTIFIEDBY:JOHNST.MARTENHQOPSOFFICER:DOUGWEAVEREMERGENCY CLASS:NOTAPPLICABLE 10CFRSECTION:CCCC21.21UNSPECIFIED PARAGRAPH JAMESNOGGLEJERRYCARTERRDONRREVENTTEXTPART21-DEFECTIVE SHUNTTRIPCOXLSTHELICENSEED1SCOVERED AWESTINGHOUSE DB-75BREAKERTHATWASFAILINGTOCLOSEATTHEIRGINNAPLANT.THEPLUNGEROFTHESHUNTTRIPCOILASSEMBLYWASBXNDING,MAINTAINING THEBREAKERTRIPPERBARINTHETRIPFREEPOSITION. | |||
THELICENSEEHASSEVENDB-75BREAKERSONSITE,ONLYONEHADTHEPROBLEMDESCRIBED. | |||
THEBREAKERWITHTHEFAILEDSHUNTTRIPCOILISTHEONLYONETOHAVEHADTHATPARTPREVIOUSLY REPLACED. | |||
THEREPLACEMENT SHUNTTR1PCOILTHATFAILEDWASONEOFTENPURCHASED IN1977ASSPARES.THEFAILEDSHUNTTRIPCOILWASREPLACEDWITHASPAREFROMSTOCK.THEREMAINING EIGHTASSEMBLIES INSTOCKWEREINSPECTED. | |||
TWOASSEMBLXES HADCOILPLUNGERSTHATDIDNOTFULLYRETURNTOTHEDEENERGIZED POSITIONDURINGMANUALMANIPULATION. | |||
THESEWEREREMOVEDFROMSTOCK.LICENSEERECOMMENDS RECEIPTINSPECTION TOVERIFYACCEPTABLE PLUNGERMOVEMENTANDALSOVERIFYING THATTHESHUNTTRIPCOILPLUNGERMOVESFREELYINTHECOILASSEMBLYDURINGBREAKERMAINTENANCE. | |||
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:~t}} | :~t}} | ||
Revision as of 10:02, 29 June 2018
| ML17309A624 | |
| Person / Time | |
|---|---|
| Site: | Ginna |
| Issue date: | 01/15/1998 |
| From: | MECREDY R C ROCHESTER GAS & ELECTRIC CORP. |
| To: | VISSING G S NRC (Affiliation Not Assigned), NRC OFFICE OF INFORMATION RESOURCES MANAGEMENT (IRM) |
| References | |
| REF-PT21-98 NUDOCS 9801220365 | |
| Download: ML17309A624 (8) | |
Text
//g(c~ROBERTC.MECREDYVicePresident NvcfeorOperotions ROCHESTER GASANDELECTRICCORPORATION
~89EASTAVENUE ROCHESTER N.Y.Id6d9.0MI AREACODE71654'6-2700 January15,1998U.S.NuclearRegulatory Commission DocumentControlDeskAttn:GuyS.VissingProjectDirectorate I-1Washington, D.C.20555
Subject:
10CFRPart2130DayReportR.E.GinnaNuclearPowerPlantDocketNo.50-244
DearMr.Vissing:
Inaccordance with10CFRPart21,Reporting ofDefectsandNoncompliance, Section21(d)(3)(ii),whichrequires"Writtennotification totheNRC...ontheidentificatiohi ofadefectorafailuretocomply",theattached10CFR21reportisherebysubmitted.
Verytrulyyours,RobertC.Mecredxc:Mr.GuyS.Vissing(MailStop14B2)ProjectDirectorate I-1DivisionofReactorProjects-I/IIOfficeofNuclearReactorRegulation U.S.NuclearRegulatory Commission Washington, D.C.20555RegionalAdministrator, RegionIU.S.NuclearRegulatory Commission 475Allendale RoadKingofPrussia,PA194066IU.S.NRCGinnaSeniorResidentInspector
'tt80i2203b5
'sI80ii5PDRADQCK05000244SPDRIIIIIII/IIIIIIIIIlIIIIIIIIIIIIIIIIIIIII h~.
10CFR2130DAYWRITTENREPORTPage2I.'AMEANDADDRESSOFTHEINDIVIDUAL INFORMING THECOMMISSION:
NAME:RobertC.Mecredy'icePresident NuclearOperations GroupADDRESS:Rochester Gas&ElectricCorporation 89.EastAvenueRochester, NewYork14649'IDENTIFICATION OFTHEFACILITY, THEACTIVITY, ORTHEBASICCOMPONENT SUPPLIEDFORSUCHFACILITYWHICHFAILSTOCOMPLYORCONTAINSADEFECT:IThefacilityistheR.E.GinnaNuclearPowerPlant.Thebasiccomponent istheshunttripassemblyonthe"B"Emergency DieselGenerator (EDG)SupplyBreakertoBus16.ThisbreakerisaWestinghouse DB-75aircircuitbreakerandtheGinnaequipment identification numberisEIN52/EG1B1, Theshunttripassemblywasinstalled onthisbreakerinMay,1995,usingsparepartspurchased in1977.IDENTIFICATION OFTHEFIRMCONSTRUCTING THEFACILITYORSUPPLYING THEBASICCOMPONENT WHICHFAILSTOCOMPLYORCONTAINSADEFECT:Theshunttripassemblywassuppliedby:Westinghouse ElectricCorporation PowerSystemsSwitchgear Division700BraddockAvenueEastPittsburgh, PA15112NATUREOFTHEDEFECTORFAILURETOCOMPLYANDTHESAFETYHAZARDWHICHISCREATEDORCOULDBECREATEDBYSUCHDEFECTORFAILURETOCOMPLY:Theshunttripcoilplungerispartoftheshunttripandalarmswitchassembly.
Theplungeroftheshunttripassemblywasbindingintheshunttripcoil.Whenactivated, thebreaker's shunttripcoilplungerpullsthebreakertripperbartotripthebreaker.Theboundplungerwasnotreturning toitsdeenergized position.
Thebreakertripperbarwasbeingmaintained inthetripfreeposition, preventing theDB-75aircircuitbreakerfromclosing.
r't,I/
Page3Testingofthe"B"EDGSupplyBreakertoBus16wasperformed inNovember, 1997,duringthe1997outage.'Duringthistesting,thebreakerfailedtoclose.Thebreakercouldnotbeclosedelectrically ormanually, becausetheshunttripcoilplungerwasmaintaining thetripperbarinthetripfreeposition.
Thisfailurewouldpreventthe"B"EDGfromsupplying powertothesafeguards loadsonBus16.Thisisconsidered amajordegradation since,inconjunction withasinglefailureontheredundant train,requiredsafetyfunctions couldnotbeperformed.
THEDATEONWHICHTHEINFORMATION OFSUCHDEFECTORFAILURETOCOMPLYWASOBTAINED:
Theinformation wasobtainedduringtestingperformed onNovember14,1997.INTHECASEOFABASICCOMPONENT WHICHCONTAINSADEFECTORFAILSTOCOMPLY,THENUMBERANDLOCATIONOFALLSUCHCOMPONENTS INUSEAT,SUPPLIEDFOR,ORBEINGSUPPLIEDFORGINNASTATION:TherearesixWestinghouse DB-75breakerspermanently installed atGinnaStation,insafeguards buses14,and16.Oneofthesebreakersismanuallyoperatedandtheshunttripcoilisnotused.Inaddition, thereisonespareDB-75breakerinstock.Withtheexception ofthe52/EG1B1breaker,thesebreakersstillhavetheiroriginalshunttripassemblies installed.
The52/EG181breakeristheonlyDB-75breakerthathashadtheshunttripassemblyreplaced.
Thereplacement shunttripassemblythatfailedwasoneoftenpurchased in1977asspares.THECORRECTIVE ACTIONWHICHHASBEEN,ISBEING,ORWILLBETAKEN;THENAMEOFTHEINDIVIDUAL ORORGANIZATION RESPONSIBLE FORTHEACTION;ANDTHELENGTHOFTIMETHATHASBEENORWILLBETAKENTOCOMPLETETHEACTION:Corrective actioniscomplete.
Thefailedshunttripassemblywasreplacedwithasparefromstock.Theassemblywasmanuallyandelectrically bench'tested priortobeingreturnedtooperablestatus.Theremaining eightassemblies instockwereinspected.
Twoassemblies hadcoilplungersthatdidnotfullyreturntothedeenergized positionduringmanualmanipulation.
Thesewereremovedfromstock.1TheotherDB-75breakerswerevisuallyinspected.
Acceptable plungermovementisindicated byadequateplungertotripperbargapandfullretraction ofthealarmswitchattachment pushrod.Noadditional bindingconcernswerefound.
Page4TheProcurement AnalysisForm(PAF)fortheshunttripassemblywasappended.
Priortoreordering, thePAFnowrequirestheadditionofplungermovementverification totheassemblyacceptance plan.Westinghouse wascontacted.
Therehavebeennootherreportedeventsofthisnature'that Westinghouse isawareof.Acheckofindustryoperational eventsdidnotidentifysimilarbreakerfailure.ANYADVICERELATEDTOTHEDEFECTORFAILURETOCOMPLYABOUTTHEFACILITY,
- ACTIVITY, ORBASICCOMPONENT THATHASBEEN,ISBEING,ORWILLBEGIVENTOPURCHASERS ORLICENSEES:
Receiptinspection couldverifyacceptable plungermovement.
DuringDB-75breakermaintenance, considerverifying thattheshunttripcoilplungermovesfreely.inthecoilbyverifying adequateplungertotripperbargapandfullretraction ofthealarmswitchattachment pushrod.
~f)JGENERALINFORMATION orOTHEREVENTNUMBER:33442LICENSEE:
ROCHESTER GASRELECTRICCORPCITY:ROCHESTER REGION:1COUNTY:STATE:NYLICENSES:
AGREEMENT:
YDOCKET:NOTIFICATXON DATE:12/22/97NOTIFICATION TIME:09:10[ET]EVENTDATE:11/14/97EVENTTIME:12:00[EST]
LASTUPDATEDATE:12/22/97NOTIFICATIONS NRCNOTIFIEDBY:JOHNST.MARTENHQOPSOFFICER:DOUGWEAVEREMERGENCY CLASS:NOTAPPLICABLE 10CFRSECTION:CCCC21.21UNSPECIFIED PARAGRAPH JAMESNOGGLEJERRYCARTERRDONRREVENTTEXTPART21-DEFECTIVE SHUNTTRIPCOXLSTHELICENSEED1SCOVERED AWESTINGHOUSE DB-75BREAKERTHATWASFAILINGTOCLOSEATTHEIRGINNAPLANT.THEPLUNGEROFTHESHUNTTRIPCOILASSEMBLYWASBXNDING,MAINTAINING THEBREAKERTRIPPERBARINTHETRIPFREEPOSITION.
THELICENSEEHASSEVENDB-75BREAKERSONSITE,ONLYONEHADTHEPROBLEMDESCRIBED.
THEBREAKERWITHTHEFAILEDSHUNTTRIPCOILISTHEONLYONETOHAVEHADTHATPARTPREVIOUSLY REPLACED.
THEREPLACEMENT SHUNTTR1PCOILTHATFAILEDWASONEOFTENPURCHASED IN1977ASSPARES.THEFAILEDSHUNTTRIPCOILWASREPLACEDWITHASPAREFROMSTOCK.THEREMAINING EIGHTASSEMBLIES INSTOCKWEREINSPECTED.
TWOASSEMBLXES HADCOILPLUNGERSTHATDIDNOTFULLYRETURNTOTHEDEENERGIZED POSITIONDURINGMANUALMANIPULATION.
THESEWEREREMOVEDFROMSTOCK.LICENSEERECOMMENDS RECEIPTINSPECTION TOVERIFYACCEPTABLE PLUNGERMOVEMENTANDALSOVERIFYING THATTHESHUNTTRIPCOILPLUNGERMOVESFREELYINTHECOILASSEMBLYDURINGBREAKERMAINTENANCE.
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