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#REDIRECT [[IR 05000155/1997005]]
{{Adams
| number = ML20149D898
| issue date = 07/14/1997
| title = Ack Receipt of Informing NRC of Steps Taken to Correct Violations Noted in Insp Rept 50-155/97-05 Completed on 970428
| author name = Grobe J
| author affiliation = NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION III)
| addressee name = Powers K
| addressee affiliation = CONSUMERS ENERGY CO. (FORMERLY CONSUMERS POWER CO.),
| docket = 05000155
| license number =
| contact person =
| document report number = 50-155-97-05, 50-155-97-5, EA-97-197, NUDOCS 9707180029
| title reference date = 06-18-1997
| document type = CORRESPONDENCE-LETTERS, OUTGOING CORRESPONDENCE
| page count = 3
}}
See also: [[see also::IR 05000155/1997005]]
 
=Text=
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July 14, 1997
EA 97-197
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Mr. K. P. Powers
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' Plant General Manager
Big Rock Point Nuclear Plant
Consumers Energy Company
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10269 US 31 North
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Charlevoix, MI 49720
4
SUBJECT:
RECEIPT OF RESPONSE TO APPARENT VIOLATIONS IN NRC INSPECTION
^
REPORT 50-155/07005(DRS)
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Dear Mr. Powers:
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This will acknowledge receipt of your letter dated June 18,1997, in response to
our letter dated May 19,1997, transmitting Inspection Report No. 50-155/97005(DRS)
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and informing you of three apparent violations resulting from three separate events at Big
Rock Point. We are currently reviewing the corrective actions described in your response
and will notify you of our enforcement decision on these matters in forthcoming
correspondence.
Sincerely,
original signed by J. M. Jacobson
John A. Grobe, Acting Director
Division of Reactor Safety
Docket No. 50-155
License No. DPR-6
Enclosure:
Ltr 6/18/97, K. P. Powers,
Consumers Energy to US NRC
DOCEMENT NAME: G:\\DRS\\ BIG 07_7.DRS
(see previous concurrence)
To receive a copy of this document, indicate in the box: "C" = Copy w/o att/enci
"E' = Copy w/att/enct
'N" = No copy
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EA 97-197
Mr. K. P. Powers
Plant General Manager
Big Rock Point Nuclear Plant
Consumers Energy Company
10269 US 31 North
Charlevoix, MI 49720
:
SUBJECT:
NOTICE OF VIOLATION (NRC INSPECTION REPORT 50-155/97005(DRS))
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Dear Mr. Powers:
,
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This will acknowledge receipt of your letter dated June 18,1997, in response to
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our letter dated May 19,1997, transmitting a Notice of Violation and informing you of
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three apparent violations resulting from three separate events at Big Rock Point. We are
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currently reviewing the corrective actions described in your response and will notify you of
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our enforcement decision on these matters in forthcoming correspondence.
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Sincerely,
3
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John A. Grobe, Acting Directc.
Division of Reactor Safety
,
Docket No. 50-155
License No. DPR-6
Enclosure:
Ltr 6/18/97, K. P. Powers,
Consumers Energy to US NRC
DOCEMENT NAME: G:\\DRS\\ BIG 07_7.DRS
To receive a copy of this document, Indicate in the box: "C" = Copy w/o atvenct T = Copy w/att/enct
'N" = No copy
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0FFICiAL RECORD COPY
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K. P. Powers
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July 14, 1997
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cc w/o encl: R. A.' Fenech, Senior Vice President,
Nuclear, Fossil, and Hydro Operations
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cc w/ encl:
James R. Padgett, Michigan Public.
Service Commission-
Michigan Department of Public Health
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Department of Attorney General (MI)
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Distribution:
Docket File w/enci
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PUBLIC IE-01 w/enct
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A. B. Beach, Rlli w/ encl
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R. Zimmerman, NRR w/enct
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A CMS Energy Company
Bg RockPonnt Nxlear Plant
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10269 US-31 hb@
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June'18, 1997
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Nuclear Regulatory Commission
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Document Control Desk
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Washington, DC
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D0CKET 50-155 - LICENSE DPR-6 - BIG ROCK POINT PLANT - RESPONSE TO APPARENT
VIOLATIONS IN INSPECTION REPORT N0. 50-155\\97005(DRS).
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_On April 28, 1997, the NRC completed a radiation protection program inspection
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at the Big Rock Point Nuclear Power Plant facility. During the inspection,
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three specific radiological control events were reviewed: a tour of the a
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high radiation area by a qualified shift supervisor and a senior radiation
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protection technician under-abnormal radiological conditions; the spread of
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contamination throughout- the turbine building durisig radioactive waste
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processing activities; and the entry into a high radiation area by a worker
who had not completed the required training for access.
Based on the results of this inspection, three apparent violations
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are being considered by the NRC for escalated enforcement action in accordance
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with the " General Statement of Policy and Procedure for NRC Enforcement
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Actions" (Enforcement Policy), NUREG-1600.
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Consumers Energy through self-assessments and event evaluations recognizes
that ti provements in the radiation protection program and plant culture are
necec ary. Our evaluations indicate that site personnel do not fully
appreciate the importance of radiation protection requirements.- Continued
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plant operation and future decomissioning activities dictate that major
improvement efforts in radiation protection are necessary.
These conclusions have lead-to a significant increase in management focus on
plant culture as it relates to radiation protection. Several staff and
department comunication meetings were targeted at plant personnel
-insensitivity to radiation protection hazards and controls. The Chemistry and
-Healthy Physics department was reorganized and resources added to improve the
radiological work control process and field monitoring.
Before the NRC decides on enforcement action, Big Rock Point staff was
provided the opportunity to either (1) respond to the apparent violations
addressed in this inspection report by June 18, 1997, or (2) request a
predecisional enforcement conference.
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NUCLEAR REGULATORY COMMISSION
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BIG ROCK POINT P,' WT
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RESPONSE TO INSPECTION 97035
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June 18, 1997
The Big Rock Point staff contacted your Mr. Thomas Kozak and notified him that
we would respond to the apparent violations in a letter in lieu of a
predecisional enforcement conference. Attached to this letter is the required
response.
Robert J Addy (Signed)
Robert J Addy
Plant Manager
CC: Administrator, Region III, USNRC
NRC Resident Inspector - Big Rock Point
ATTACHMENT
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CONSUMERS ENERGY COMPANY
To the best of my knowledge, information and belief, the contents of this
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submittal are truthful and complete.
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By Robert J Addy (Sioned)
Robert J Addy
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Plant Manager
Sworn and subscribed to before me this 18th day of June 1997.
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Jennifer Lynn Helms (Sioned)
Jennifer Lynn Helms, Notary Public
Charlevoix County, Michigan
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My commission expires August 29, 1999.
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ATTACHMENT
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CONSUNERS ENERGY CONPANY
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BIG ROCK P0 INT PLANT
DOCKET 50-155
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DOCKET 50-155 - LICENSE DPR-6 - BIG ROCK POINT PLANT - RESPONSE TO APPARENT
VIOLATIONS IN INSPECTION REPORT NO. 50-155\\97005(DRS).
Submitted June 18, 1997
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RESPONSE TO APPARENT VIOLATIONS IN INSPECTION REPORT 97005
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ESCALATED ENFORCEMENT ITEM 50-155/97005-01a
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10 CFR Part 20.1501, requires licensee's to make surveys that are reasonable
under the circumstances to evaluate the extent of radiation levels and the
potential radiological hazards that could be present.
The failure of the
workers to evaluate the extent of radiation levels and the potential
radiological hazards that could be present (gamma dose rates ranged up to 7
renv' hour and the neutron dose rates ranged up to 1.5 rea/ hour during the grand
tour) to ensure compliance with 10 CFR 20.1201(a)(1), is an apparent violation
of 10 CFR 20.1501(a) (EEI 50-155/97005-01a).
ESCALATED ENFORCEMENT ITEM 50-155/97005-02a
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Failuru to exit the HRA after receiving electronic dosinetry alaras during the
grand tour is an example of an apparent violation of Technical Specification
(TS) 6.11.
This TS refers to Administrative Procedure 5.8, "High Radiation
Area Key and Access Control," Revision 10, which requires in Step 5.1.f.7.
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that a HRA be fanediately exited on either an ED dose or dose rate alarm (EEI
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50-155/97005-02a).
Consumers Energy Company agrees with the apparent violations as assessed.
(1) The reason for the aooarent violations.
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A team investigation concluded the station was exhibiting a casual
approach to radiation protection and radiation work practices.
The radiation work permit (RWP) did not adequately characterize
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the actual radiological conditions in the areas being inspected.
Historical data that was readily available was not utilized. For
example,'the maximum dose rate-general area, indicated on the RWP
was 2 Rem / hour. Actual general area dose rates of 6 - 7 Rem / hour
gamma and 1.5 Rem /hr neutron existed in the area. The RWP
reflected plant shutdown conditions, but the tour was conducted
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during low power operation.
The RWP did not clearly define the neutron monitoring
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requirements. As a result, based on the initial neutron survey in
the lower recirculation pump room, both individuals thought that
the neutron dose rate along the inspection path was approximately
180 mrem / hour. However, the actual neutron dose rate in the steam
drum area was approximately 1500 mrem / hour.
The dose rate and entry dose level (EDL) alarms identified on the
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RWP were inappropriate for the actual conditions. The dose rate
alarm was set at 3 Rem / hour and the entry dose level (EDL) alarm
was set at 100 mrem.
Previous low power radiological data for the
-area shows dose rates in excess of 3 Rem / hour in the areas. Al so,
previous experience conducting tours shows that 150 to 300 mrem is
typically received.
The As low As Reasonably Achievable (ALARA) planning for the
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inspection was superficial and did not consider several key
factors, such as the route to be followed and previous at-power
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entry dose rates.
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The job planning and the prejob briefing with respect to
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Operations Department activities did not address ALARA or the
radiological conditions expected in the area.
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'.f . RESPONSE To APPAREN1 VIOLATIONS IN INSPECTION REPORT 97005
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The individuals involved did not adequately review and understand
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the RWP co1ditions and requirements.
For example, the personnel
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knew that a 100 mrem entry dose level (EDL) was probably too low
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for the task, but did not question the limit.
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Requirements and expectations for procedure adherence were not well
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understood by station personnel.
In this case, both individuals knew
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the requirement upon receiving a dose rate or entry dose level (EDL)
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alarm, but they did not follow through with the proper action.
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Both individuals received the dose rate alam while climbing the
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ladder to the steam drum area.
They should have stopped and
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exited the area upon ' receiving the alam, but they proceeded on.
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Shortly thereafter, both received an entry dose level (EDL) alarm,
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then discussed their situation and decided to continue with the
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inspection to avoid a subsequent entry. The expectation is clear
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on receiving an entry dose level (EDL) alare: stop, exit the ares
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and contact radiation protection personnel.
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Senior management, department managers and first line supervision were
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not sufficiently involved in the radiological aspects of this type of
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operations activity to ensure the proper focus and attention is directed
to the planning and execution of these evolutions.
In this specific
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event, management was not sensitive to the need for or the precautions
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required to be taken for an at-power entry " grand tour" into the
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recirculation pump room.
Further, several opportunities to correct the
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deficiencies in the planning of this inspection, such as in the
development of the RWP, the conduct of the prejob brief, and the
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communication of dose rate monitoring expectations, were missed because
senior management was not meaningfully involved.
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(2) The corrective steos that have been taken and the results achieved.
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Immediate
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A.
The Plant Manager immediately required an interim measure making his
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approval necessary prior to performing work in a high radiation area.
Further, all radiation work permits were rereviewed and received
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Chemistry / Health Physics Manager's approval.
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B.
The appropriate discipline was administered to the two individuals
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involved in the event.
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Short Term
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-The lessons learned from this event were communicated to all plant
personnel by March 4,1997 via a memorandum from the Plant Manager to
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all station personnel. The memo addressed the casual approach adopted by
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all station personnel concerning radiation protection, procedural
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adherence inadequacies and inadequate management attention to important
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plant work. These expectations were personally presented to the
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management staff by the Plant Manager. The event and expectations were
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also discussed with the radiological protection, maintenance,
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operations, and other appropriate on-site personnel by the management
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staff with the assistance of Health Physics management.
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, RESPONSE TO APPARENT VIOLATIONS IN INSPECTION REPORT 97005
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B.
On March 1,1997, the Chemistry / Health Physics department was
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reorganized to improve supervisory coaching and oversight; and improve
radiation protection technician support in the technician and ALARA
planning functions. Two new supervisory positions were added to improve
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the-planning and implementation of radiation protection work. Three
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additional technicians have been contracted. Further, one additional
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technician was added to the staff to improve ALARA work planning.
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The Chemistry / Health Physics Manager developed a performance enhancement
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plan to address the deficiencies identified with the RWP preparation and
RP preplanning for this event. The plan also addresses radiation
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protection equipment requirements and needs.
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(3) The corrective stens that will be taken to avoid further violations.
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A.
A case study will be developed and presented to all radiation workers on
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the lessons learned from this event. The purpose of this case study will
be to emphasize management's expectation for procedure adherence,
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commitment to ALARA, and the need to improve the radiation work permit
and radiation work practices.
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THIS ACTION WILL BE COMPLETED BY SEPTEN8ER 1, 1997.
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B.
Enhanced training in RWP preparation and radiation protection coverage
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techniques including dose reduction techniques will be conducted by the
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Chemistry / Health Physics Manager. Radiation protection equipment
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requirements and needs will also be discussed.
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THIS ACTION WILL BE COMPLETED BY SEPTEM8ER 1, 1997.
(4) The date when full comoliance will be achieved.
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The facility is currently in full compliance.
ESCALATED ENFORCEMENT ITEN 50-155/97005-01b
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Although pre-job and ALARA reviews were performed prior to the filter transfer
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job, insufficiant attention was given to the changed plant and radiological
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conditions such as the ventilation systen being placed in a cold weather
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configuration, higher than normal dose rates on the filters, and the longer
storage time for the filters which allowed then to dry out making it much more
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likely that contanination would become airborne. Because HRA work was on
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hold, the filters began to accumulate in the RWPA causing the higher than
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usual dose rates, and the filters had dried out for a month compared to a
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normal week or two. A significant airborne radioactive material condition
resulted when the filters were transferred without the use of engineering
controls.
The failure to properly evaluate the potential radiological hazards
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associated with the transfer of the highly contaminated filters is an
additional example of an apparent violation of 10 CFR 20.1501(a). (EEI No. 50-
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15SH7005-01b).
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Consumers Energy Company agrees with the apparent violations as assessed.
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(1) The reason for the aooarent violations.
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The major cause for this violation is the failure of the radiological planning
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and control processes to adequately account for changes in work methods.
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Other contributing factors were also involved.
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The radioactive waste filter barrel (RWFB) was installed in the spring of 1996
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in order to provide a temporary overflow location for filters when the
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radioactive waste filter cask (RWFC) became full and there were more filters
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requiring change before transport to the radwaste building could be
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accomplished. Prior to installing the RWFB, excess filters had been placed in
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plastic bags and lain on the floor. The bagged filters that had to be
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recovered manually from within the radioactive waste room at significant
expense of dose. The RWFB allowed filter transfer into the RWFC remotely (long
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handled pole) from above. The evolution resulted in approximately 15 person-
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mrem as compared to approximately 150 person-area when the filters were
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individually bagged. Because radioactive waste disposal site criteria limit
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the water content of shipped waste, the new RWFB is perforated to allow
drainage. It is not covered purposely to allow ease of filter additions
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(covering and uncovering would add time and therefore dose during use). The
open and perforated configuration promotes drying.
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Transfer of filters from the RWFB to the RWFC caused no airborne radioactivity
problems throughout 1996. The latest barrel to cask transfer prior to the
event on February 24, 1997, appears to have been on September 26, 1996. After
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the S ptember,1996 date, filters were transported to the radioactive waste
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bui16ing directly by use of the transfer cask (barrel is used only for
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overflow, and was not necessary). The last such direct transport was on
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January 24, 1997. After that, the RWFC was filled and the RWFB started to be
used when the High Radiation Area Radiation Work permits (RWPs) went on hold
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due to the EDL incident on January 31, 1997. The next direct transport of
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filters occurred just prior to the transfer incident (in order to empty the
transfer cask so that the filters from the barrel could then be transferred to
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the cask). The transport went without incident.
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The RWFC holds about 24 filters, and the overflow RWFB holds approximately 96.
The barrels are currently empty,
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The transfer between the RWFB and transport cask performed February 24, 1997,
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appears to be the first time such transfers have been performed under " cold
weather" conditions with most or all outside air louvers closed. Since the
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flow went through the turbine building rather than to the stack plenum as
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indicated in plant drawings, it appears that air flow under the current
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ventilation mode caused the problem of contamination spread in the turbine
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building.
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Additional information pertinent to this event is provided in the response to
apparent violation 50-155/97005-03.
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(2) The corrective steos that have been taken and the results achieved.
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The radioactive waste damper was aligned to provide the correct ventilation
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flowpath (i.e., negative pressure for the filter area). Flow was verified by
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the use of a smoke generator. The Chemistry / Health Physics work control group
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established controls and barriers within the procedure and radiation work
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permit to accomplish the transfer. A safety evaluation was completed to review
barriers and plant configuration. Since the realignment of the ventilation
system, casks have been successfully loaded and transferred to the radwaste
building,
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Drying of the filters contributed to the problem by creating loose radioactive
particles available for transport. This has been controlled by use of a gentle
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spray mist to dampen filter surfaces. Use of a local High Efficiency
Particulate (HEPA) filter has also been implemented. The cefling plug, which
used to be opened to allow manipulation of the filters from above, will now
remain closed. New tools have been purchased that allow the filters to changed
f, rom within the room.
(3) The corrective steos that will be taken to avoid further violations.
No further actions will be taken. The action taken above 'as adequately
addressed the plant's filter change process.
(4) The date when full como11ance will be achieved.
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The facility is currently in full compliance.
ESCALATED ENFORCEMENT ITEN 50-155/97005-02b
On January 20,1997,' the licensee identified that a station engineer who was
not high radiation area access (HRAA) qualified entered the reactor water
clean up pump roon on two occasions. Although he was accompanied by an
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auxiliary operator who was HRAA qualified, this was not in acconiance with
Administrative Procedure 5.8.c, 'HRA Key and Access Control," which states
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that entry into HRAs is not allowed unless there are two persons, both of whom
should be HRAA qualified, and if one person is not, then he/she will be
provided with dedicated RPT coverage.
The area entered was posted and
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controlled as a HRA with sone sections having general area dose rates in
excess of 1 ren/hr.
The failure of the non-qualified engineer to be provided
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with RPT coverage is an additional example of an apparent violation of TS 6.11
requirements that radiation protection procedures be established and adhered
to.
(EEI No. 50-155/97005-02b).
Consumers Energy Company agrees with the apparent violation as assessed.
(1) The reason for the aooarent violation.
The cause of this event is similar in nature to EEI No. 50-155/97-02a. In
particular, the lack of sensitivity of station personnel to the radiological
aspects of work at the station, and radiological interfaces with plant
activities resulted in this incident.
(2) The corrective steos that have been taken and the results achieved.
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Station management reorganized and enhanced the Chemistry / Health Physics
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organization to address the station issue of lack of sensitivity to radiation
protection and the radiological planning process. A Chemistry / Health Physics
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work control line function was established to review all plant work, improve
the inadequacies identified in RWP preparation, integrate RP into the plant
planning process and plan the radiological aspects of plant work. Thresholds
for job coverage, formal and informal briefings have been lowered. An up-to-
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RESPONSE TO APPARENT VIOLATIONS IN INSPECTION REPORT 97005
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A
date listing of High Radiation Area Access (HRAA) qualified individuals is
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maintained and readily available for verification of HRAA qualification.
!
Further, an industry experienced Chemistry / Health Physics planner position and
an additional supervisor was added to the staff. These additions will provide
immediate assistance for planning the radiological aspects of station work,
,
J
and management oversight in the field will be enhanced.
[
Station management communicated the incident to the plant staff through
;
briefings with Chemistry / Health Physics and Engineering personnel, and a
i
comprehensive memorandum to all plant personnel was issued by the Plant
i
Nanager. Individuals involved in the incident were also counseled as to the
j
expectations associated with this incident.
i
!
(3) The corrective steos that will be taken to avoid further violations.
}
j
A.
A case study will be developed and presented to all radiation workers on
:
the lessons learned from the events identified in 50-155/97005-0!a and
'
50-155/97005-02a. The purpose of this case study will be to emphasize
;
management's expectation for procedure adherence, comitment to ALARA,
and the need to improve the radiation work permit and radiation work
,
j
practices.
1
THIS ACTION WILL BE COMPLETED BY SEPTEMBER 1, 1997.
.
4
l
B.
Enhanced training in RWP preparation and radiation protection coverage
techniques including dose reduction techniques will be conducted by the
1
i
Chemistry / Health Physics Manager. Radiation protection equipment
j
requirements and needs will also be discussed.
!
THIS ACTION WILL BE COMPLETED BY SEPTEMBER 1, 1997.
i
j
(4) The date when full como11ance will be achieved.
.
I
The facility is currently in full compliance.
P
ESCALATED ENFORCEMENT ITEM 50-155/97005-03
.
,
.
.
The gaseous waste management systen description in Final Hazards Safety Report
i
(FHSR), Section 11.3.2, states that air flow rates will remain sufficient to
)
minimize build-up of airborne contanination and that flows begin in
^
radioactively clean areas and are directed to potentially more highly
l'
contaminated areas then exhausted to the stack. Drawing number 0740G40124,
i
which is referenced in FHSR Section 11.3.2, indicates that air flows from the
;
RWPA directly into the exhaust plenum and out the plant stack.
During this
'
event, the air flow was reversed (from the RWPA through the turbine butiding,
1
into the pipe tunnel, and out the main stack).
This flow was from an area of
i
high contamination to one of lower contamination levels. During the
licensee's investigation of the event, the danper on the RWPA exhaust plenun
i
)
was found to be closed (this was not expected even in a cold weather
3
configuration), thereby considerably restricting the air flow of the exhaust
i
systen, which caused the flow to reverse.
It was not determined when or how
long the damper had been closed.
This nodification to the air flow pathway
<
i
was not adequately analyzed. No design change or 10 CFR 50.59 safety
evaluation was performed to address the new ventilation flow path.
This is
;
considered an example of an apparent violation of 10 CFR 50.59 (EEI No. 50-
155/97005-03(DRS)).
!
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RESPONSE TO APPARENT VIOLATIONS IN INSPECTION REPORT 97005
-
7
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Consumers Energy Company agrees with the apparent violation as assessed.
(1) The reason for the aooarent violations.
The position of the damper was not adequately controlled by procedure.
Previous filter transfers had not resulted in contamination problems;
therefore, the need for procedural control had not been recognized and the
:
associated design considerations made. Additional detail on the circumstances
;
;
surrounding this event is provided in the response to apparent violation 50-
'
155/97005-Olb.
(2)Thecorrectivesteosthathavebeentakenandtheresultsachieved.
,
The past method of transfer was discontinued and the use of additional
engineering controls was established.
Including changing the method of
transfer from a stabbing to a grasping action with shorter tools that do not
i
'
require removal of the ceiling plug.
The damper position was reestablished
and a 50.59 evaluation performed on its as-left position.
(3) The corrective steos that will be taken to avoid further violations.
.
Big Rock Point has recognized that existing procedures may lack specific
guidance for addressing all of the possible plant configurations.
Recent
4
management emphasis on procedure compliance and adequacy is stressing the need
to assure proper plant configuration and procedure revision, when necessary to
maintain it.
(4) The date when full compliance will be achieved.
i
The facility is currently in full compliance.
i
l
.
i
}}

Latest revision as of 17:08, 24 May 2025

Ack Receipt of Informing NRC of Steps Taken to Correct Violations Noted in Insp Rept 50-155/97-05 Completed on 970428
ML20149D898
Person / Time
Site: Big Rock Point File:Consumers Energy icon.png
Issue date: 07/14/1997
From: Grobe J
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION III)
To: Powers K
CONSUMERS ENERGY CO. (FORMERLY CONSUMERS POWER CO.)
References
50-155-97-05, 50-155-97-5, EA-97-197, NUDOCS 9707180029
Download: ML20149D898 (3)


See also: IR 05000155/1997005

Text

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,

July 14, 1997

EA 97-197

!

Mr. K. P. Powers

!

' Plant General Manager

Big Rock Point Nuclear Plant

Consumers Energy Company

'

10269 US 31 North

'

Charlevoix, MI 49720

4

SUBJECT:

RECEIPT OF RESPONSE TO APPARENT VIOLATIONS IN NRC INSPECTION

^

REPORT 50-155/07005(DRS)

i

Dear Mr. Powers:

i

This will acknowledge receipt of your letter dated June 18,1997, in response to

our letter dated May 19,1997, transmitting Inspection Report No. 50-155/97005(DRS)

i

and informing you of three apparent violations resulting from three separate events at Big

Rock Point. We are currently reviewing the corrective actions described in your response

and will notify you of our enforcement decision on these matters in forthcoming

correspondence.

Sincerely,

original signed by J. M. Jacobson

John A. Grobe, Acting Director

Division of Reactor Safety

Docket No. 50-155

License No. DPR-6

Enclosure:

Ltr 6/18/97, K. P. Powers,

Consumers Energy to US NRC

DOCEMENT NAME: G:\\DRS\\ BIG 07_7.DRS

(see previous concurrence)

To receive a copy of this document, indicate in the box: "C" = Copy w/o att/enci

"E' = Copy w/att/enct

'N" = No copy

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EA 97-197

Mr. K. P. Powers

Plant General Manager

Big Rock Point Nuclear Plant

Consumers Energy Company

10269 US 31 North

Charlevoix, MI 49720

SUBJECT:

NOTICE OF VIOLATION (NRC INSPECTION REPORT 50-155/97005(DRS))

i

Dear Mr. Powers:

,

4

This will acknowledge receipt of your letter dated June 18,1997, in response to

i

l

our letter dated May 19,1997, transmitting a Notice of Violation and informing you of

i

three apparent violations resulting from three separate events at Big Rock Point. We are

i

.

currently reviewing the corrective actions described in your response and will notify you of

our enforcement decision on these matters in forthcoming correspondence.

j'

Sincerely,

3

1,

John A. Grobe, Acting Directc.

Division of Reactor Safety

,

Docket No. 50-155

License No. DPR-6

Enclosure:

Ltr 6/18/97, K. P. Powers,

Consumers Energy to US NRC

DOCEMENT NAME: G:\\DRS\\ BIG 07_7.DRS

To receive a copy of this document, Indicate in the box: "C" = Copy w/o atvenct T = Copy w/att/enct

'N" = No copy

0FFICE

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K. P. Powers

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July 14, 1997

'

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cc w/o encl: R. A.' Fenech, Senior Vice President,

Nuclear, Fossil, and Hydro Operations

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cc w/ encl:

James R. Padgett, Michigan Public.

Service Commission-

Michigan Department of Public Health

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Department of Attorney General (MI)

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Distribution:

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PUBLIC IE-01 w/enct

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A. B. Beach, Rlli w/ encl

J. Goldberg, OGC w/enci

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Rlli Enf. Coordinator w/enci

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A CMS Energy Company

Bg RockPonnt Nxlear Plant

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10269 US-31 hb@

Ptant GeneralManager

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June'18, 1997

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Nuclear Regulatory Commission

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Document Control Desk

Washington, DC

20555

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D0CKET 50-155 - LICENSE DPR-6 - BIG ROCK POINT PLANT - RESPONSE TO APPARENT

VIOLATIONS IN INSPECTION REPORT N0. 50-155\\97005(DRS).

,

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_On April 28, 1997, the NRC completed a radiation protection program inspection

1

at the Big Rock Point Nuclear Power Plant facility. During the inspection,

i

three specific radiological control events were reviewed: a tour of the a

i

high radiation area by a qualified shift supervisor and a senior radiation

[

protection technician under-abnormal radiological conditions; the spread of

l

contamination throughout- the turbine building durisig radioactive waste

i

processing activities; and the entry into a high radiation area by a worker

who had not completed the required training for access.

Based on the results of this inspection, three apparent violations

i

are being considered by the NRC for escalated enforcement action in accordance

j

with the " General Statement of Policy and Procedure for NRC Enforcement

i

Actions" (Enforcement Policy), NUREG-1600.

'

Consumers Energy through self-assessments and event evaluations recognizes

that ti provements in the radiation protection program and plant culture are

necec ary. Our evaluations indicate that site personnel do not fully

appreciate the importance of radiation protection requirements.- Continued

^

plant operation and future decomissioning activities dictate that major

improvement efforts in radiation protection are necessary.

These conclusions have lead-to a significant increase in management focus on

plant culture as it relates to radiation protection. Several staff and

department comunication meetings were targeted at plant personnel

-insensitivity to radiation protection hazards and controls. The Chemistry and

-Healthy Physics department was reorganized and resources added to improve the

radiological work control process and field monitoring.

Before the NRC decides on enforcement action, Big Rock Point staff was

provided the opportunity to either (1) respond to the apparent violations

addressed in this inspection report by June 18, 1997, or (2) request a

predecisional enforcement conference.

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NUCLEAR REGULATORY COMMISSION

2

'

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BIG ROCK POINT P,' WT

.

RESPONSE TO INSPECTION 97035

l-

June 18, 1997

The Big Rock Point staff contacted your Mr. Thomas Kozak and notified him that

we would respond to the apparent violations in a letter in lieu of a

predecisional enforcement conference. Attached to this letter is the required

response.

Robert J Addy (Signed)

Robert J Addy

Plant Manager

CC: Administrator, Region III, USNRC

NRC Resident Inspector - Big Rock Point

ATTACHMENT

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CONSUMERS ENERGY COMPANY

To the best of my knowledge, information and belief, the contents of this

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submittal are truthful and complete.

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By Robert J Addy (Sioned)

Robert J Addy

i

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Plant Manager

Sworn and subscribed to before me this 18th day of June 1997.

!

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Jennifer Lynn Helms (Sioned)

Jennifer Lynn Helms, Notary Public

Charlevoix County, Michigan

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My commission expires August 29, 1999.

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ATTACHMENT

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CONSUNERS ENERGY CONPANY

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BIG ROCK P0 INT PLANT

DOCKET 50-155

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DOCKET 50-155 - LICENSE DPR-6 - BIG ROCK POINT PLANT - RESPONSE TO APPARENT

VIOLATIONS IN INSPECTION REPORT NO. 50-155\\97005(DRS).

Submitted June 18, 1997

,

_

_..

_.__ _ _ .

_ _ _ _ _ _ _ _ _ _ _ _ _ . _ _ _ _ _ _ _ _ _ _ _ _

'

RESPONSE TO APPARENT VIOLATIONS IN INSPECTION REPORT 97005

.

-

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,

ESCALATED ENFORCEMENT ITEM 50-155/97005-01a

1

'

-

10 CFR Part 20.1501, requires licensee's to make surveys that are reasonable

under the circumstances to evaluate the extent of radiation levels and the

potential radiological hazards that could be present.

The failure of the

workers to evaluate the extent of radiation levels and the potential

radiological hazards that could be present (gamma dose rates ranged up to 7

renv' hour and the neutron dose rates ranged up to 1.5 rea/ hour during the grand

tour) to ensure compliance with 10 CFR 20.1201(a)(1), is an apparent violation

of 10 CFR 20.1501(a) (EEI 50-155/97005-01a).

ESCALATED ENFORCEMENT ITEM 50-155/97005-02a

l

Failuru to exit the HRA after receiving electronic dosinetry alaras during the

grand tour is an example of an apparent violation of Technical Specification (TS) 6.11.

This TS refers to Administrative Procedure 5.8, "High Radiation

Area Key and Access Control," Revision 10, which requires in Step 5.1.f.7.

r

l

that a HRA be fanediately exited on either an ED dose or dose rate alarm (EEI

\\

50-155/97005-02a).

Consumers Energy Company agrees with the apparent violations as assessed.

(1) The reason for the aooarent violations.

A team investigation concluded the station was exhibiting a casual

approach to radiation protection and radiation work practices.

The radiation work permit (RWP) did not adequately characterize

.

the actual radiological conditions in the areas being inspected.

Historical data that was readily available was not utilized. For

example,'the maximum dose rate-general area, indicated on the RWP

was 2 Rem / hour. Actual general area dose rates of 6 - 7 Rem / hour

gamma and 1.5 Rem /hr neutron existed in the area. The RWP

reflected plant shutdown conditions, but the tour was conducted

,

l

during low power operation.

The RWP did not clearly define the neutron monitoring

.

requirements. As a result, based on the initial neutron survey in

the lower recirculation pump room, both individuals thought that

the neutron dose rate along the inspection path was approximately

180 mrem / hour. However, the actual neutron dose rate in the steam

drum area was approximately 1500 mrem / hour.

The dose rate and entry dose level (EDL) alarms identified on the

.

RWP were inappropriate for the actual conditions. The dose rate

alarm was set at 3 Rem / hour and the entry dose level (EDL) alarm

was set at 100 mrem.

Previous low power radiological data for the

-area shows dose rates in excess of 3 Rem / hour in the areas. Al so,

previous experience conducting tours shows that 150 to 300 mrem is

typically received.

The As low As Reasonably Achievable (ALARA) planning for the

.

inspection was superficial and did not consider several key

factors, such as the route to be followed and previous at-power

j

entry dose rates.

(

The job planning and the prejob briefing with respect to

.

Operations Department activities did not address ALARA or the

radiological conditions expected in the area.

.

,

.

.

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_ _ _ _ . _ _ _ _ _ _ _ _ . . _ _ _ _ . . - _ _ __. _ ..

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.

'.f . RESPONSE To APPAREN1 VIOLATIONS IN INSPECTION REPORT 97005

,

-

.

'

5

2

The individuals involved did not adequately review and understand

r

.

!

the RWP co1ditions and requirements.

For example, the personnel

!

knew that a 100 mrem entry dose level (EDL) was probably too low

i

for the task, but did not question the limit.

'

Requirements and expectations for procedure adherence were not well

,

understood by station personnel.

In this case, both individuals knew

I

'

the requirement upon receiving a dose rate or entry dose level (EDL)

alarm, but they did not follow through with the proper action.

'

i

Both individuals received the dose rate alam while climbing the

.

ladder to the steam drum area.

They should have stopped and

j

exited the area upon ' receiving the alam, but they proceeded on.

Shortly thereafter, both received an entry dose level (EDL) alarm,

j

then discussed their situation and decided to continue with the

inspection to avoid a subsequent entry. The expectation is clear

-

on receiving an entry dose level (EDL) alare: stop, exit the ares

i

and contact radiation protection personnel.

l

Senior management, department managers and first line supervision were

!

not sufficiently involved in the radiological aspects of this type of

l

operations activity to ensure the proper focus and attention is directed

to the planning and execution of these evolutions.

In this specific

event, management was not sensitive to the need for or the precautions

required to be taken for an at-power entry " grand tour" into the

recirculation pump room.

Further, several opportunities to correct the

1

deficiencies in the planning of this inspection, such as in the

development of the RWP, the conduct of the prejob brief, and the

communication of dose rate monitoring expectations, were missed because

senior management was not meaningfully involved.

j

(2) The corrective steos that have been taken and the results achieved.

i

Immediate

i

A.

The Plant Manager immediately required an interim measure making his

1

approval necessary prior to performing work in a high radiation area.

Further, all radiation work permits were rereviewed and received

l

Chemistry / Health Physics Manager's approval.

!

B.

The appropriate discipline was administered to the two individuals

!

involved in the event.

!

Short Term

A.

-The lessons learned from this event were communicated to all plant

personnel by March 4,1997 via a memorandum from the Plant Manager to

i

all station personnel. The memo addressed the casual approach adopted by

i

j

all station personnel concerning radiation protection, procedural

adherence inadequacies and inadequate management attention to important

i

plant work. These expectations were personally presented to the

.

management staff by the Plant Manager. The event and expectations were

j

also discussed with the radiological protection, maintenance,

j

operations, and other appropriate on-site personnel by the management

j

staff with the assistance of Health Physics management.

l-

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, RESPONSE TO APPARENT VIOLATIONS IN INSPECTION REPORT 97005

,

'*

.

I

3

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j

i

B.

On March 1,1997, the Chemistry / Health Physics department was

!

reorganized to improve supervisory coaching and oversight; and improve

radiation protection technician support in the technician and ALARA

planning functions. Two new supervisory positions were added to improve

^

'

the-planning and implementation of radiation protection work. Three

i

additional technicians have been contracted. Further, one additional

technician was added to the staff to improve ALARA work planning.

i

C.

The Chemistry / Health Physics Manager developed a performance enhancement

i

plan to address the deficiencies identified with the RWP preparation and

RP preplanning for this event. The plan also addresses radiation

i

protection equipment requirements and needs.

,

,

(3) The corrective stens that will be taken to avoid further violations.

l

A.

A case study will be developed and presented to all radiation workers on

'

.

the lessons learned from this event. The purpose of this case study will

be to emphasize management's expectation for procedure adherence,

3

commitment to ALARA, and the need to improve the radiation work permit

and radiation work practices.

THIS ACTION WILL BE COMPLETED BY SEPTEN8ER 1, 1997.

$

B.

Enhanced training in RWP preparation and radiation protection coverage

.

techniques including dose reduction techniques will be conducted by the

l

Chemistry / Health Physics Manager. Radiation protection equipment

j

requirements and needs will also be discussed.

4

j

THIS ACTION WILL BE COMPLETED BY SEPTEM8ER 1, 1997.

(4) The date when full comoliance will be achieved.

<

The facility is currently in full compliance.

ESCALATED ENFORCEMENT ITEN 50-155/97005-01b

Although pre-job and ALARA reviews were performed prior to the filter transfer

.

job, insufficiant attention was given to the changed plant and radiological

-

conditions such as the ventilation systen being placed in a cold weather

-

'

configuration, higher than normal dose rates on the filters, and the longer

storage time for the filters which allowed then to dry out making it much more

j

likely that contanination would become airborne. Because HRA work was on

i

hold, the filters began to accumulate in the RWPA causing the higher than

.

j

usual dose rates, and the filters had dried out for a month compared to a

'

normal week or two. A significant airborne radioactive material condition

resulted when the filters were transferred without the use of engineering

controls.

The failure to properly evaluate the potential radiological hazards

associated with the transfer of the highly contaminated filters is an

additional example of an apparent violation of 10 CFR 20.1501(a). (EEI No. 50-

i

15SH7005-01b).

,

Consumers Energy Company agrees with the apparent violations as assessed.

I

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  • ,' .' . RESPONSE TO APPARENT VIOLATIONS IN INSPECTION REPORT 97005

-

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4

(1) The reason for the aooarent violations.

!

!

The major cause for this violation is the failure of the radiological planning

,

and control processes to adequately account for changes in work methods.

l

Other contributing factors were also involved.

.

'

The radioactive waste filter barrel (RWFB) was installed in the spring of 1996

!

in order to provide a temporary overflow location for filters when the

!

radioactive waste filter cask (RWFC) became full and there were more filters

{

requiring change before transport to the radwaste building could be

i

accomplished. Prior to installing the RWFB, excess filters had been placed in

j

plastic bags and lain on the floor. The bagged filters that had to be

i

recovered manually from within the radioactive waste room at significant

expense of dose. The RWFB allowed filter transfer into the RWFC remotely (long

i

handled pole) from above. The evolution resulted in approximately 15 person-

!

mrem as compared to approximately 150 person-area when the filters were

i

individually bagged. Because radioactive waste disposal site criteria limit

l

the water content of shipped waste, the new RWFB is perforated to allow

drainage. It is not covered purposely to allow ease of filter additions

i

(covering and uncovering would add time and therefore dose during use). The

open and perforated configuration promotes drying.

3

l

Transfer of filters from the RWFB to the RWFC caused no airborne radioactivity

problems throughout 1996. The latest barrel to cask transfer prior to the

event on February 24, 1997, appears to have been on September 26, 1996. After

j

the S ptember,1996 date, filters were transported to the radioactive waste

.

bui16ing directly by use of the transfer cask (barrel is used only for

8

overflow, and was not necessary). The last such direct transport was on

January 24, 1997. After that, the RWFC was filled and the RWFB started to be

used when the High Radiation Area Radiation Work permits (RWPs) went on hold

i

due to the EDL incident on January 31, 1997. The next direct transport of

l

filters occurred just prior to the transfer incident (in order to empty the

transfer cask so that the filters from the barrel could then be transferred to

'

the cask). The transport went without incident.

1

The RWFC holds about 24 filters, and the overflow RWFB holds approximately 96.

The barrels are currently empty,

i

The transfer between the RWFB and transport cask performed February 24, 1997,

{

appears to be the first time such transfers have been performed under " cold

weather" conditions with most or all outside air louvers closed. Since the

i

flow went through the turbine building rather than to the stack plenum as

'

j

indicated in plant drawings, it appears that air flow under the current

ventilation mode caused the problem of contamination spread in the turbine

j

building.

l

Additional information pertinent to this event is provided in the response to

apparent violation 50-155/97005-03.

'

3

(2) The corrective steos that have been taken and the results achieved.

l

The radioactive waste damper was aligned to provide the correct ventilation

i

flowpath (i.e., negative pressure for the filter area). Flow was verified by

i

the use of a smoke generator. The Chemistry / Health Physics work control group

j

established controls and barriers within the procedure and radiation work

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permit to accomplish the transfer. A safety evaluation was completed to review

barriers and plant configuration. Since the realignment of the ventilation

system, casks have been successfully loaded and transferred to the radwaste

building,

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Drying of the filters contributed to the problem by creating loose radioactive

particles available for transport. This has been controlled by use of a gentle

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spray mist to dampen filter surfaces. Use of a local High Efficiency

Particulate (HEPA) filter has also been implemented. The cefling plug, which

used to be opened to allow manipulation of the filters from above, will now

remain closed. New tools have been purchased that allow the filters to changed

f, rom within the room.

(3) The corrective steos that will be taken to avoid further violations.

No further actions will be taken. The action taken above 'as adequately

addressed the plant's filter change process.

(4) The date when full como11ance will be achieved.

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The facility is currently in full compliance.

ESCALATED ENFORCEMENT ITEN 50-155/97005-02b

On January 20,1997,' the licensee identified that a station engineer who was

not high radiation area access (HRAA) qualified entered the reactor water

clean up pump roon on two occasions. Although he was accompanied by an

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auxiliary operator who was HRAA qualified, this was not in acconiance with

Administrative Procedure 5.8.c, 'HRA Key and Access Control," which states

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that entry into HRAs is not allowed unless there are two persons, both of whom

should be HRAA qualified, and if one person is not, then he/she will be

provided with dedicated RPT coverage.

The area entered was posted and

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controlled as a HRA with sone sections having general area dose rates in

excess of 1 ren/hr.

The failure of the non-qualified engineer to be provided

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with RPT coverage is an additional example of an apparent violation of TS 6.11

requirements that radiation protection procedures be established and adhered

to.

(EEI No. 50-155/97005-02b).

Consumers Energy Company agrees with the apparent violation as assessed.

(1) The reason for the aooarent violation.

The cause of this event is similar in nature to EEI No. 50-155/97-02a. In

particular, the lack of sensitivity of station personnel to the radiological

aspects of work at the station, and radiological interfaces with plant

activities resulted in this incident.

(2) The corrective steos that have been taken and the results achieved.

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Station management reorganized and enhanced the Chemistry / Health Physics

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organization to address the station issue of lack of sensitivity to radiation

protection and the radiological planning process. A Chemistry / Health Physics

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work control line function was established to review all plant work, improve

the inadequacies identified in RWP preparation, integrate RP into the plant

planning process and plan the radiological aspects of plant work. Thresholds

for job coverage, formal and informal briefings have been lowered. An up-to-

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RESPONSE TO APPARENT VIOLATIONS IN INSPECTION REPORT 97005

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date listing of High Radiation Area Access (HRAA) qualified individuals is

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maintained and readily available for verification of HRAA qualification.

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Further, an industry experienced Chemistry / Health Physics planner position and

an additional supervisor was added to the staff. These additions will provide

immediate assistance for planning the radiological aspects of station work,

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and management oversight in the field will be enhanced.

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Station management communicated the incident to the plant staff through

briefings with Chemistry / Health Physics and Engineering personnel, and a

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comprehensive memorandum to all plant personnel was issued by the Plant

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Nanager. Individuals involved in the incident were also counseled as to the

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expectations associated with this incident.

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(3) The corrective steos that will be taken to avoid further violations.

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A.

A case study will be developed and presented to all radiation workers on

the lessons learned from the events identified in 50-155/97005-0!a and

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50-155/97005-02a. The purpose of this case study will be to emphasize

management's expectation for procedure adherence, comitment to ALARA,

and the need to improve the radiation work permit and radiation work

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practices.

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THIS ACTION WILL BE COMPLETED BY SEPTEMBER 1, 1997.

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Enhanced training in RWP preparation and radiation protection coverage

techniques including dose reduction techniques will be conducted by the

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Chemistry / Health Physics Manager. Radiation protection equipment

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requirements and needs will also be discussed.

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THIS ACTION WILL BE COMPLETED BY SEPTEMBER 1, 1997.

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(4) The date when full como11ance will be achieved.

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The facility is currently in full compliance.

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ESCALATED ENFORCEMENT ITEM 50-155/97005-03

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The gaseous waste management systen description in Final Hazards Safety Report

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(FHSR), Section 11.3.2, states that air flow rates will remain sufficient to

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minimize build-up of airborne contanination and that flows begin in

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radioactively clean areas and are directed to potentially more highly

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contaminated areas then exhausted to the stack. Drawing number 0740G40124,

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which is referenced in FHSR Section 11.3.2, indicates that air flows from the

RWPA directly into the exhaust plenum and out the plant stack.

During this

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event, the air flow was reversed (from the RWPA through the turbine butiding,

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into the pipe tunnel, and out the main stack).

This flow was from an area of

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high contamination to one of lower contamination levels. During the

licensee's investigation of the event, the danper on the RWPA exhaust plenun

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was found to be closed (this was not expected even in a cold weather

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configuration), thereby considerably restricting the air flow of the exhaust

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systen, which caused the flow to reverse.

It was not determined when or how

long the damper had been closed.

This nodification to the air flow pathway

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was not adequately analyzed. No design change or 10 CFR 50.59 safety

evaluation was performed to address the new ventilation flow path.

This is

considered an example of an apparent violation of 10 CFR 50.59 (EEI No. 50-

155/97005-03(DRS)).

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RESPONSE TO APPARENT VIOLATIONS IN INSPECTION REPORT 97005

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Consumers Energy Company agrees with the apparent violation as assessed.

(1) The reason for the aooarent violations.

The position of the damper was not adequately controlled by procedure.

Previous filter transfers had not resulted in contamination problems;

therefore, the need for procedural control had not been recognized and the

associated design considerations made. Additional detail on the circumstances

surrounding this event is provided in the response to apparent violation 50-

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155/97005-Olb.

(2)Thecorrectivesteosthathavebeentakenandtheresultsachieved.

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The past method of transfer was discontinued and the use of additional

engineering controls was established.

Including changing the method of

transfer from a stabbing to a grasping action with shorter tools that do not

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require removal of the ceiling plug.

The damper position was reestablished

and a 50.59 evaluation performed on its as-left position.

(3) The corrective steos that will be taken to avoid further violations.

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Big Rock Point has recognized that existing procedures may lack specific

guidance for addressing all of the possible plant configurations.

Recent

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management emphasis on procedure compliance and adequacy is stressing the need

to assure proper plant configuration and procedure revision, when necessary to

maintain it.

(4) The date when full compliance will be achieved.

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The facility is currently in full compliance.

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