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{{#Wiki_filter:October 19, 2007
{{#Wiki_filter:October 19, 2007
Richard M. Rosenblum
Richard M. Rosenblum  
Senior Vice President and
Senior Vice President and  
   Chief Nuclear Officer
   Chief Nuclear Officer
Southern California Edison Company
Southern California Edison Company
San Onofre Nuclear Generating Station
San Onofre Nuclear Generating Station
P.O. Box 128
P.O. Box 128
San Clemente, CA 92674-0128
San Clemente, CA 92674-0128    
SUBJECT: SAN ONOFRE NUCLEAR GENERATING STATION - NRC SPECIAL
SUBJECT:
              INSPECTION REPORT 05000361/2007013; 05000362/2007013
SAN ONOFRE NUCLEAR GENERATING STATION - NRC SPECIAL
INSPECTION REPORT 05000361/2007013; 05000362/2007013
Dear Mr. Rosenblum:
Dear Mr. Rosenblum:
On September 13, 2007, the U.S. Nuclear Regulatory Commission (NRC) completed a special
On September 13, 2007, the U.S. Nuclear Regulatory Commission (NRC) completed a special
inspection at your San Onofre Nuclear Generating Station facility. This inspection examined
inspection at your San Onofre Nuclear Generating Station facility. This inspection examined
activities associated with the loss of instrument air event on June 20, 2007. On this occasion,
activities associated with the loss of instrument air event on June 20, 2007. On this occasion,
instrument air pressure on Unit 2 dropped significantly, causing the feedwater control valves to
instrument air pressure on Unit 2 dropped significantly, causing the feedwater control valves to
stop functioning and resulting in an increase in steam generator water level. Operators
stop functioning and resulting in an increase in steam generator water level. Operators
manually tripped the Unit 2 reactor. The NRC's initial evaluation satisfied the criteria in NRC
manually tripped the Unit 2 reactor. The NRC's initial evaluation satisfied the criteria in NRC
Management Directive 8.3, NRC Incident Investigation Program, for conducting a special
Management Directive 8.3, NRC Incident Investigation Program, for conducting a special
inspection. The basis for initiating this special inspection is further discussed in the inspection
inspection. The basis for initiating this special inspection is further discussed in the inspection
charter, which is included in this report as Attachment 2. The determination that the inspection
charter, which is included in this report as Attachment 2. The determination that the inspection
would be conducted was made by the NRC on June 26, 2007, and the inspection started on
would be conducted was made by the NRC on June 26, 2007, and the inspection started on
June 27, 2007.
June 27, 2007.
The enclosed inspection report documents the inspection findings, which were discussed on
The enclosed inspection report documents the inspection findings, which were discussed on
September 13, 2007 and again on October 11, 2007, with members of your staff. The
September 13, 2007 and again on October 11, 2007, with members of your staff. The
inspection examined activities conducted under your license as they relate to safety and
inspection examined activities conducted under your license as they relate to safety and
compliance with the Commission's rules and regulations and with the conditions of your license.
compliance with the Commission's rules and regulations and with the conditions of your license.  
The inspectors reviewed selected procedures and records, observed activities, and interviewed
The inspectors reviewed selected procedures and records, observed activities, and interviewed
personnel.
personnel.
The report documents eight NRC identified and self-revealing findings of very low safety
The report documents eight NRC identified and self-revealing findings of very low safety
significance (Green). The eight findings involved issues concerning both the failure of your
significance (Green). The eight findings involved issues concerning both the failure of your
processes and programs to prevent or mitigate the loss of instrument air event, and the
processes and programs to prevent or mitigate the loss of instrument air event, and the
subsequent failure of your staff to thoroughly evaluate operator and equipment responses
subsequent failure of your staff to thoroughly evaluate operator and equipment responses
following the event. The NRC is concerned about the occurrence of this event and the less
following the event. The NRC is concerned about the occurrence of this event and the less
than adequate reviews conducted by your staff, and will conduct followup baseline inspections
than adequate reviews conducted by your staff, and will conduct followup baseline inspections
to verify that your corrective actions in response to this inspection are thorough and effective.
to verify that your corrective actions in response to this inspection are thorough and effective.  
Five of the findings were determined to involve violations of NRC requirements. Because of
Five of the findings were determined to involve violations of NRC requirements. Because of
their very low safety significance and because they were entered into your corrective action
their very low safety significance and because they were entered into your corrective action
program, the NRC is treating these findings as noncited violations (NCVs) consistent with
program, the NRC is treating these findings as noncited violations (NCVs) consistent with
Section VI.A.1 of the NRC Enforcement Policy. If you contest these NCVs, you should provide
Section VI.A.1 of the NRC Enforcement Policy.   If you contest these NCVs, you should provide


Southern California Edison Company             -2-
Southern California Edison Company
- 2 -
a response within 30 days of the date of this inspection report, with the basis for your denial, to
a response within 30 days of the date of this inspection report, with the basis for your denial, to
the U.S. Nuclear Regulatory Commission, ATTN: Document Control Desk, Washington
the U.S. Nuclear Regulatory Commission, ATTN: Document Control Desk, Washington
DC 20555-0001; with copies to the Regional Administrator, U.S. Nuclear Regulatory
DC 20555-0001; with copies to the Regional Administrator, U.S. Nuclear Regulatory
Commission Region IV, 611 Ryan Plaza Drive, Suite 400, Arlington, Texas, 76011-4005; the
Commission Region IV, 611 Ryan Plaza Drive, Suite 400, Arlington, Texas, 76011-4005; the
Director, Office of Enforcement, U.S. Nuclear Regulatory Commission, Washington
Director, Office of Enforcement, U.S. Nuclear Regulatory Commission, Washington
Line 68: Line 70:
enclosure, and your response (if any) will be made available electronically for public inspection
enclosure, and your response (if any) will be made available electronically for public inspection
in the NRC Public Document Room or from the Publicly Available Records (PARS) component
in the NRC Public Document Room or from the Publicly Available Records (PARS) component
of NRCs document system (ADAMS). ADAMS is accessible from the NRC Web site at
of NRCs document system (ADAMS). ADAMS is accessible from the NRC Web site at
http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room).
http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room).
                                            Sincerely,
Sincerely,
                                            /RA/
/RA/
                                            Jeffrey A. Clark, Chief
Jeffrey A. Clark, Chief
                                            Projects Branch E
Projects Branch E
                                            Division of Reactor Projects
Division of Reactor Projects
Dockets: 50-361
Dockets:   50-361
          50-362
    50-362
License: NPF-10
License: NPF-10
          NPF-15
    NPF-15
Enclosure: Inspection Report 05000361/2007013; 05000362/2007013
Enclosure: Inspection Report 05000361/2007013; 05000362/2007013
   Attachment 1: Supplemental Information
   Attachment 1: Supplemental Information
   Attachment 2: Special Inspection Charter
   Attachment 2: Special Inspection Charter
   Attachment 3: Significance Determination Evaluation
   Attachment 3: Significance Determination Evaluation
cc w/Enclosure:
cc w/Enclosure:
Chairman, Board of Supervisors                       Dr. David Spath, Chief
Chairman, Board of Supervisors
County of San Diego                                 Division of Drinking Water and
County of San Diego
1600 Pacific Highway, Room 335                       Environmental Management
1600 Pacific Highway, Room 335
San Diego, CA 92101                                 California Department of Health Services
San Diego, CA 92101
                                                    850 Marina Parkway, Bldg P, 2nd Floor
Gary L. Nolff
Gary L. Nolff                                       Richmond, CA 94804
Assistant Director-Resources
Assistant Director-Resources
City of Riverside                                   Michael J. DeMarco
City of Riverside
3900 Main Street                                     San Onofre Liaison
3900 Main Street
Riverside, CA 92522                                 San Diego Gas & Electric Company
Riverside, CA 92522
                                                    8315 Century Park Ct. CP21G
Mark L. Parsons
Mark L. Parsons                                     San Diego, CA 92123-1548
Deputy City Attorney
Deputy City Attorney
City of Riverside                                   Director, Radiological Health Branch
City of Riverside
3900 Main Street                                    State Department of Health Services
3900 Main Street
Riverside, CA 92522                                  P.O. Box 997414 (MS 7610)
Riverside, CA  92522
                                                    Sacramento, CA 95899-7414
Dr. David Spath, Chief
Division of Drinking Water and
  Environmental Management
California Department of Health Services
850 Marina Parkway, Bldg P, 2nd Floor
Richmond, CA 94804
Michael J. DeMarco
San Onofre Liaison
San Diego Gas & Electric Company
8315 Century Park Ct. CP21G
San Diego, CA  92123-1548
Director, Radiological Health Branch
State Department of Health Services
P.O. Box 997414 (MS 7610)
Sacramento, CA 95899-7414


Southern California Edison Company   -3-
Southern California Edison Company
Mayor
- 3 -
Mayor  
City of San Clemente
City of San Clemente
100 Avenida Presidio
100 Avenida Presidio
San Clemente, CA 92672
San Clemente, CA 92672
James D. Boyd, Commissioner
James D. Boyd, Commissioner
California Energy Commission
California Energy Commission
1516 Ninth Street (MS 34)
1516 Ninth Street (MS 34)
Sacramento, CA 95814
Sacramento, CA 95814
Douglas K. Porter, Esq.
Douglas K. Porter, Esq.
Southern California Edison Company
Southern California Edison Company
2244 Walnut Grove Avenue
2244 Walnut Grove Avenue
Rosemead, CA 91770
Rosemead, CA 91770
Mr. Raymond W. Waldo, Vice President,
Mr. Raymond W. Waldo, Vice President,
Nuclear Generation
Nuclear Generation
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San Onofre Nuclear Generating Station
San Onofre Nuclear Generating Station
P.O. Box 128
P.O. Box 128
San Clemente, CA 92674-0128
San Clemente, CA 92674-0128
A. Edward Scherer
A. Edward Scherer
Southern California Edison Company
Southern California Edison Company
San Onofre Nuclear Generating Station
San Onofre Nuclear Generating Station
P.O. Box 128
P.O. Box 128
San Clemente, CA 92674-0128
San Clemente, CA 92674-0128
Brian Katz
Brian Katz
Southern California Edison Company
Southern California Edison Company
San Onofre Nuclear Generating Station
San Onofre Nuclear Generating Station
P.O. Box 128
P.O. Box 128
San Clemente, CA 92674-0128
San Clemente, CA 92674-0128
Mr. Steve Hsu
Mr. Steve Hsu
Department of Health Services
Department of Health Services
Line 136: Line 151:
MS 7610, P.O. Box 997414
MS 7610, P.O. Box 997414
Sacramento, CA 95899-7414
Sacramento, CA 95899-7414
Mr. James T. Reilly
Mr. James T. Reilly
Southern California Edison Company
Southern California Edison Company
San Onofre Nuclear Generating Station
San Onofre Nuclear Generating Station
Line 142: Line 157:
San Clemente, CA 92674-0128
San Clemente, CA 92674-0128


Southern California Edison Company             -4-
Southern California Edison Company
- 4 -
Electronic distribution by RIV:
Electronic distribution by RIV:
Regional Administrator (EEC)
Regional Administrator (EEC)
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DRS STA (DAP)
DRS STA (DAP)
V. Dricks, PAO (VLD)
V. Dricks, PAO (VLD)
D. Pelton, OEDO RIV Coordinator (DLP)
D. Pelton, OEDO RIV Coordinator (DLP)
ROPreports
ROPreports
SO Site Secretary (vacant)
SO Site Secretary (vacant)
SUNSI Review Completed: _JAC__           ADAMS: : Yes G No       Initials: __JAC_
SUNSI Review Completed: _JAC__     ADAMS: : Yes
: Publicly Available      G Non-Publicly Available  G Sensitive       : Non-Sensitive
G No       Initials: __JAC_  
R:\_REACTORS\SO\2007\SO2007-13RP-GBM.wpd
:   Publicly Available      G   Non-Publicly Available     G   Sensitive
RIV:SRI:DRP/C RI:DRP/E                 SRI:DRP/E     SRA:DRS           C:DRP/E
:   Non-Sensitive
GBMiller             JEJosey           CCOsterholtz   DPLoveless         JAClark
R:\\_REACTORS\\SO\\2007\\SO2007-13RP-GBM.wpd                        
        /RA/         T-GBM             E=GBM         /RA/               /RA/
RIV:SRI:DRP/C
10/16 /07           10/17/07         10/16/07       10/17/07           10/19/07
RI:DRP/E
OFFICIAL RECORD COPY                                 T=Telephone         E=E-mail   F=Fax
SRI:DRP/E
SRA:DRS
C:DRP/E
GBMiller
JEJosey
CCOsterholtz
DPLoveless
JAClark
/RA/
T-GBM
   
   
E=GBM
/RA/
/RA/
10/16 /07
10/17/07
10/16/07
10/17/07
10/19/07
OFFICIAL RECORD COPY  
T=Telephone           E=E-mail       F=Fax


              U.S. NUCLEAR REGULATORY COMMISSION
Enclosure
                                REGION IV
-1-
Docket:     50-361, 50-362
U.S. NUCLEAR REGULATORY COMMISSION  
Licenses:   NPF-10, NPF-15
REGION IV  
Report No.: 05000361/2007013; 05000362/2007013
Docket:
Licensee:   Southern California Edison Co. (SCE)
50-361, 50-362
Facility:   San Onofre Nuclear Generating Station, Units 2, 3
Licenses:
Location:   5000 S. Pacific Coast Hwy.
NPF-10, NPF-15
            San Clemente, California
Report No.:
Dates:       June 27 through September 13, 2007
05000361/2007013; 05000362/2007013
Inspectors: J. Josey, Resident Inspector, Project Branch E, DRP
Licensee:
            D. Loveless, Senior Reactor Analyst
Southern California Edison Co. (SCE)
            G. Miller, Senior Resident Inspector, Project Branch C, DRP
Facility:
            C. Osterholtz, Senior Resident Inspector, Project Branch E, DRP
San Onofre Nuclear Generating Station, Units 2, 3
            M. Sitek, Resident Inspector, Project Branch E, DRP
Location:
Approved By: Jeffrey A. Clark, Chief
5000 S. Pacific Coast Hwy.  
            Project Branch E
San Clemente, California  
            Division of Reactor Projects
Dates:
                                    -1-                                  Enclosure
June 27 through September 13, 2007
Inspectors:
J. Josey, Resident Inspector, Project Branch E, DRP
D. Loveless, Senior Reactor Analyst
G. Miller, Senior Resident Inspector, Project Branch C, DRP
C. Osterholtz, Senior Resident Inspector, Project Branch E, DRP
M. Sitek, Resident Inspector, Project Branch E, DRP
Approved By:
Jeffrey A. Clark, Chief
Project Branch E
Division of Reactor Projects


                                        SUMMARY OF FINDINGS
Enclosure
-2-
SUMMARY OF FINDINGS
IR 05000361/2007013, 05000362/2007013; 06/27/07 - 07/02/07; San Onofre Nuclear
IR 05000361/2007013, 05000362/2007013; 06/27/07 - 07/02/07; San Onofre Nuclear
Generating Station, Units 2, 3, and Independent Spent Fuel Storage Installation; Special
Generating Station, Units 2, 3, and Independent Spent Fuel Storage Installation; Special
Line 194: Line 243:
The report covered a 6-day period (June 27 - July 2, 2007) of onsite inspection, with inoffice
The report covered a 6-day period (June 27 - July 2, 2007) of onsite inspection, with inoffice
review through September 13, 2007, by a special inspection team consisting of one senior
review through September 13, 2007, by a special inspection team consisting of one senior
resident inspector, one resident inspector, and one senior reactor analyst. Eight findings were
resident inspector, one resident inspector, and one senior reactor analyst. Eight findings were
identified. The significance of most findings is indicated by its color (Green, White, Yellow, or
identified. The significance of most findings is indicated by its color (Green, White, Yellow, or
Red) using Inspection Manual Chapter 0609, Significance Determination Process. Findings
Red) using Inspection Manual Chapter 0609, Significance Determination Process. Findings
for which the significance determination process does not apply may be Green or be assigned a
for which the significance determination process does not apply may be Green or be assigned a
severity level after NRCs management review. The NRC's program for overseeing the safe
severity level after NRCs management review. The NRC's program for overseeing the safe
operation of commercial nuclear power reactors is described in NUREG-1649, Reactor
operation of commercial nuclear power reactors is described in NUREG-1649, Reactor
Oversight Process, Revision 3, dated July 2000.
Oversight Process, Revision 3, dated July 2000.
Summary of Event
Summary of Event
The NRC conducted a special inspection to better understand the circumstances surrounding
The NRC conducted a special inspection to better understand the circumstances surrounding
an instrument air header break and Unit 2 trip on June 20, 2007. In accordance with NRC
an instrument air header break and Unit 2 trip on June 20, 2007. In accordance with NRC
Management Directive 8.3, NRC Incident Investigation Program, it was determined that this
Management Directive 8.3, NRC Incident Investigation Program, it was determined that this
event involved multiple failures in systems used to mitigate the effects of an actual event,
event involved multiple failures in systems used to mitigate the effects of an actual event,
involved potential adverse generic implications, and had sufficient risk significance to warrant a
involved potential adverse generic implications, and had sufficient risk significance to warrant a
special inspection.
special inspection.  
A.       NRC-Identified and Self-Revealing Findings
A.
        Cornerstone: Initiating Events
NRC-Identified and Self-Revealing Findings
        *   Green. The inspectors reviewed a self-revealing Green finding involving
Cornerstone: Initiating Events
              ineffective corrective actions taken in response to site and industry operating
*
              experience with instrument air header ruptures. Specifically, contrary to
Green. The inspectors reviewed a self-revealing Green finding involving
              Section 6.2.3 of Procedure SO-123-I-1.42, Maintenance Division Experience
ineffective corrective actions taken in response to site and industry operating
              Report, Revision 0, the licensee failed to implement corrective actions to prevent
experience with instrument air header ruptures. Specifically, contrary to
              recurrence for an equipment failure with the potential to cause a significant plant
Section 6.2.3 of Procedure SO-123-I-1.42, Maintenance Division Experience
              transient, and failed to appropriately consider previous industry and plant
Report, Revision 0, the licensee failed to implement corrective actions to prevent
              experience similar to the event. Additionally, licensee personnel failed to properly
recurrence for an equipment failure with the potential to cause a significant plant
              evaluate and take corrective actions based on industry operating experience
transient, and failed to appropriately consider previous industry and plant
              through 2006 involving improperly made soldered joints in instrument air systems.
experience similar to the event. Additionally, licensee personnel failed to properly
              As a result, an additional failure of an improperly made instrument air header joint
evaluate and take corrective actions based on industry operating experience
              occurred at SONGS on June 20, 2007. The licensee entered this issue in their
through 2006 involving improperly made soldered joints in instrument air systems.  
              corrective action program as Action Request AR 070600867.
As a result, an additional failure of an improperly made instrument air header joint
              This finding was more than minor since it was associated with the equipment
occurred at SONGS on June 20, 2007. The licensee entered this issue in their
              reliability attribute of the initiating events cornerstone and affected the cornerstone
corrective action program as Action Request AR 070600867.
              objective to limit the likelihood of events that upset plant stability and challenge
This finding was more than minor since it was associated with the equipment
              critical safety functions. This finding required a Phase 2 analysis per the Manual
reliability attribute of the initiating events cornerstone and affected the cornerstone
              Chapter 0609, Significance Determination Process, Phase 1 Worksheets since
objective to limit the likelihood of events that upset plant stability and challenge
              the loss of instrument air is a transient initiator resulting in the loss of the
critical safety functions. This finding required a Phase 2 analysis per the Manual
              feedwater system which is part of the power conversion system which can be used
Chapter 0609, Significance Determination Process, Phase 1 Worksheets since
              to mitigate the consequences of an accident. Based on the results of the Phase 2
the loss of instrument air is a transient initiator resulting in the loss of the
                                                      -2-                                      Enclosure
feedwater system which is part of the power conversion system which can be used
to mitigate the consequences of an accident. Based on the results of the Phase 2  


    analysis and a subsequent Phase 3 analysis, the finding was determined to be of
Enclosure
    very low safety significance (Green) because of the availability of the diverse
-3-
    auxiliary feedwater system and the ability of the operators to depressurize the
analysis and a subsequent Phase 3 analysis, the finding was determined to be of
    steam generators and utilize the condensate system for heat removal. These
very low safety significance (Green) because of the availability of the diverse
    results were evaluated by a senior reactor analyst. This finding has a crosscutting
auxiliary feedwater system and the ability of the operators to depressurize the
    aspect in the area of problem identification and resolution associated with
steam generators and utilize the condensate system for heat removal. These
    operating experience in that the licensee failed to effectively implement changes to
results were evaluated by a senior reactor analyst. This finding has a crosscutting
    station processes, procedures, and equipment in response to operating
aspect in the area of problem identification and resolution associated with
    experience involving improperly made instrument air system joints [P.2(b)].
operating experience in that the licensee failed to effectively implement changes to
    (Section 2.1)
station processes, procedures, and equipment in response to operating
*   Green. The inspectors identified a Green noncited violation of Technical
experience involving improperly made instrument air system joints [P.2(b)].  
    Specification 5.5.1.1 involving the failure to meet procedural requirements
(Section 2.1)
    following a loss of instrument air. Specifically, operators failed to monitor nitrogen
*
    tank levels or take precautions for the possibility of oxygen-deficient areas in the
Green. The inspectors identified a Green noncited violation of Technical
    plant following actuation of the low pressure backup nitrogen system. The
Specification 5.5.1.1 involving the failure to meet procedural requirements
    licensee entered this issue in their corrective action program as Action
following a loss of instrument air. Specifically, operators failed to monitor nitrogen
    Request AR 070700291.
tank levels or take precautions for the possibility of oxygen-deficient areas in the
    This finding was more than minor since it was associated with the human
plant following actuation of the low pressure backup nitrogen system. The
    performance attribute of the initiating events cornerstone and affected the
licensee entered this issue in their corrective action program as Action
    cornerstone objective to limit the likelihood of events that upset plant stability and
Request AR 070700291.
    challenge critical safety functions. This finding required a Phase 2 analysis in
This finding was more than minor since it was associated with the human
    accordance with the Manual Chapter 0609, Significance Determination Process,
performance attribute of the initiating events cornerstone and affected the
    Phase 1 Worksheets since the loss of instrument air is a transient initiator resulting
cornerstone objective to limit the likelihood of events that upset plant stability and
    in the loss of the feedwater system which is part of the power conversion system
challenge critical safety functions. This finding required a Phase 2 analysis in
    which can be used to mitigate the consequences of an accident. Based on the
accordance with the Manual Chapter 0609, Significance Determination Process,
    results of the Phase 2 analysis, the finding was determined to be of very low safety
Phase 1 Worksheets since the loss of instrument air is a transient initiator resulting
    significance because of the low likelihood of a complete loss of instrument air and
in the loss of the feedwater system which is part of the power conversion system
    the availability of the auxiliary feedwater system. The cause of this finding has a
which can be used to mitigate the consequences of an accident. Based on the
    crosscutting aspect in the area of human performance associated with resources
results of the Phase 2 analysis, the finding was determined to be of very low safety
    because licensee personnel were not adequately trained on the operation of the
significance because of the low likelihood of a complete loss of instrument air and
    low pressure nitrogen system to effectively implement the abnormal operating
the availability of the auxiliary feedwater system. The cause of this finding has a
    instruction [H.2(b)]. (Section 2.2)
crosscutting aspect in the area of human performance associated with resources
because licensee personnel were not adequately trained on the operation of the
low pressure nitrogen system to effectively implement the abnormal operating
instruction [H.2(b)]. (Section 2.2)
Cornerstone: Mitigating Systems
Cornerstone: Mitigating Systems
*   Green. A self-revealing, Green noncited violation of 10 CFR Part 50, Appendix B,
*
    Criterion III, Design Control, was identified when Unit 2 experienced a loss of
Green. A self-revealing, Green noncited violation of 10 CFR Part 50, Appendix B,
    instrument air due to the failure of a soldered joint. Specifically, the loss of
Criterion III, Design Control, was identified when Unit 2 experienced a loss of
    instrument air resulted in component cooling water (CCW) Pump 024 being in a
instrument air due to the failure of a soldered joint. Specifically, the loss of
    runout condition for approximately 75 minutes due to a previous system
instrument air resulted in component cooling water (CCW) Pump 024 being in a
    modification. The licensee entered this issue in their corrective action program as
runout condition for approximately 75 minutes due to a previous system
    Action Requests AR 070700051 and 070600872.
modification. The licensee entered this issue in their corrective action program as
    This finding was greater than minor because it was associated with the mitigating
Action Requests AR 070700051 and 070600872.
    systems cornerstone attribute of design control and affected the associated
This finding was greater than minor because it was associated with the mitigating
    cornerstone objective to ensure the availability, reliability, and capability of systems
systems cornerstone attribute of design control and affected the associated
    that respond to initiating events to prevent undesirable consequences. The finding
cornerstone objective to ensure the availability, reliability, and capability of systems
    did not affect the initiating events cornerstone functions of the component cooling
that respond to initiating events to prevent undesirable consequences. The finding
    water system because the condition would only have existed given a loss of
did not affect the initiating events cornerstone functions of the component cooling
                                          -3-                                      Enclosure
water system because the condition would only have existed given a loss of


  instrument air initiator had already occurred. In accordance with NRC Inspection
Enclosure
  Manual Chapter 0609, Appendix A, Phase 1 Worksheet, Significance
-4-
  Determination Process (SDP) Phase 1 Screening Worksheet for the Initiating
instrument air initiator had already occurred. In accordance with NRC Inspection
  Events, Mitigating Systems, and Barriers Cornerstones, this finding was
Manual Chapter 0609, Appendix A, Phase 1 Worksheet, Significance
  determined to be of very low safety significance because the finding was a design
Determination Process (SDP) Phase 1 Screening Worksheet for the Initiating
  deficiency confirmed not to result in a loss of operability per Part 9900, Technical
Events, Mitigating Systems, and Barriers Cornerstones, this finding was
  Guidance, Operability Determination Process for Operability and Functional
determined to be of very low safety significance because the finding was a design
  Assessment. (Section 2.3)
deficiency confirmed not to result in a loss of operability per Part 9900, Technical
* Green. The inspectors reviewed a self-revealing Green finding involving the failure
Guidance, Operability Determination Process for Operability and Functional
  to take effective corrective actions for a failed control room annunciator.
Assessment. (Section 2.3)
  Specifically, after the annunciator for actuation of the backup nitrogen supply to
*
  the instrument air system failed to function on demand on several occasions from
Green. The inspectors reviewed a self-revealing Green finding involving the failure
  1994 through 2007, the corrective actions taken by the licensee to restore the
to take effective corrective actions for a failed control room annunciator.  
  annunciator to service were inadequate and narrowly focused. The annunciator
Specifically, after the annunciator for actuation of the backup nitrogen supply to
  subsequently failed to function during the loss of instrument air event on
the instrument air system failed to function on demand on several occasions from
  June 20, 2007. The licensee entered this issue in their corrective action program
1994 through 2007, the corrective actions taken by the licensee to restore the
  as Action Request AR 070601250.
annunciator to service were inadequate and narrowly focused. The annunciator
  This finding was more than minor since it was associated with the human
subsequently failed to function during the loss of instrument air event on
  performance attribute of the initiating events cornerstone and affected the
June 20, 2007. The licensee entered this issue in their corrective action program
  cornerstone objective to limit the likelihood of events that upset plant stability and
as Action Request AR 070601250.
  challenge critical safety functions. This finding required a Phase 2 analysis in
This finding was more than minor since it was associated with the human
  accordance with the Manual Chapter 0609, Significance Determination Process,
performance attribute of the initiating events cornerstone and affected the
  Phase 1 Worksheets since the loss of instrument air is a transient initiator resulting
cornerstone objective to limit the likelihood of events that upset plant stability and
  in the loss of the feedwater system which is part of the power conversion system
challenge critical safety functions. This finding required a Phase 2 analysis in
  which can be used to mitigate the consequences of an accident. Based on the
accordance with the Manual Chapter 0609, Significance Determination Process,
  results of the Phase 2 analysis, the finding was determined to be of very low safety
Phase 1 Worksheets since the loss of instrument air is a transient initiator resulting
  significance because of the low likelihood of a complete loss of instrument air and
in the loss of the feedwater system which is part of the power conversion system
  the availability of the auxiliary feedwater system. This finding has a crosscutting
which can be used to mitigate the consequences of an accident. Based on the
  aspect in the area of problem identification and resolution associated with the
results of the Phase 2 analysis, the finding was determined to be of very low safety
  corrective action program in that the licensee failed to thoroughly evaluate the
significance because of the low likelihood of a complete loss of instrument air and
  failed annunciator such that the resolution appropriately addressed the causes
the availability of the auxiliary feedwater system. This finding has a crosscutting
  [P.2(c)]. (Section 2.4)
aspect in the area of problem identification and resolution associated with the
* Green. The inspectors identified a Green noncited violation of Technical
corrective action program in that the licensee failed to thoroughly evaluate the
  Specification 5.5.1.1 involving the failure to maintain an adequate abnormal
failed annunciator such that the resolution appropriately addressed the causes
  operating instruction for a loss of instrument air event. The licensee entered this
[P.2(c)]. (Section 2.4)
  issue in their corrective action program as Action Request AR 070801151.
*
  This finding was more than minor because it was associated with the procedure
Green. The inspectors identified a Green noncited violation of Technical
  quality attribute of the mitigating systems cornerstone and affected the
Specification 5.5.1.1 involving the failure to maintain an adequate abnormal
  cornerstone objective to ensure the availability, reliability and capability of systems
operating instruction for a loss of instrument air event. The licensee entered this
  that respond to initiating events, in that a less than adequate abnormal operating
issue in their corrective action program as Action Request AR 070801151.
  procedure could have prevented operators from promptly tripping the reactor,
This finding was more than minor because it was associated with the procedure
  allowing conditions to continue to degrade and resulting in a demand on the
quality attribute of the mitigating systems cornerstone and affected the
  reactor protection system. Using the Significance Determination Process Phase 1
cornerstone objective to ensure the availability, reliability and capability of systems
  Screening Worksheet in Appendix A of Inspection Manual Chapter 0609, the
that respond to initiating events, in that a less than adequate abnormal operating
  inspectors determined this finding had very low safety significance because it did
procedure could have prevented operators from promptly tripping the reactor,
  not result in an actual loss of safety function per Part 9900, Technical Guidance,
allowing conditions to continue to degrade and resulting in a demand on the
  Operability Determination Process for Operability and Functional Assessment.
reactor protection system. Using the Significance Determination Process Phase 1
                                      -4-                                      Enclosure
Screening Worksheet in Appendix A of Inspection Manual Chapter 0609, the
inspectors determined this finding had very low safety significance because it did
not result in an actual loss of safety function per Part 9900, Technical Guidance,
Operability Determination Process for Operability and Functional Assessment.  


  This finding has a crosscutting aspect in the area of human performance
Enclosure
  associated with resources in that the licensee failed to provide operators with
-5-
  complete, accurate, and up-to-date procedures [H.2(c)]. (Section 2.5)
This finding has a crosscutting aspect in the area of human performance
* Green. A self-revealing, Green noncited violation of 10 CFR Part 55.46(c)(1) was
associated with resources in that the licensee failed to provide operators with
  identified involving the licensees failure to incorporate a design change in
complete, accurate, and up-to-date procedures [H.2(c)]. (Section 2.5)
  modeling plant response for the plant-referenced simulator. Specifically, during
*
  operator training in the plant-referenced simulator, the controlled bleedoff valves
Green. A self-revealing, Green noncited violation of 10 CFR Part 55.46(c)(1) was
  for the reactor coolant pumps were modeled to fail closed on a loss of instrument
identified involving the licensees failure to incorporate a design change in
  air, whereas the valves in the plant remained open during an actual loss of
modeling plant response for the plant-referenced simulator. Specifically, during
  instrument air event on June 20, 2007. The licensee entered this issue in their
operator training in the plant-referenced simulator, the controlled bleedoff valves
  corrective action program as Action Requests AR 070600873 and 070900160.
for the reactor coolant pumps were modeled to fail closed on a loss of instrument
  This finding was greater than minor because it was associated with the mitigating
air, whereas the valves in the plant remained open during an actual loss of
  systems cornerstone attribute of human performance and affected the associated
instrument air event on June 20, 2007. The licensee entered this issue in their
  cornerstone objective to ensure the availability, reliability, and capability of systems
corrective action program as Action Requests AR 070600873 and 070900160.
  that respond to initiating events to prevent undesirable consequences. The
This finding was greater than minor because it was associated with the mitigating
  inspectors evaluated this finding using the Appendix I, Licensed Operator
systems cornerstone attribute of human performance and affected the associated
  Requalification Significance Determination Process worksheets of Manual
cornerstone objective to ensure the availability, reliability, and capability of systems
  Chapter 0609 because the finding is a requalification training issue related to
that respond to initiating events to prevent undesirable consequences. The
  simulator fidelity. The finding is of very low safety significance because the
inspectors evaluated this finding using the Appendix I, Licensed Operator
  discrepancy did not have an adverse impact on operator actions such that safety
Requalification Significance Determination Process worksheets of Manual
  related equipment was made inoperable during normal operations or in response
Chapter 0609 because the finding is a requalification training issue related to
  to a plant transient. This finding has a crosscutting aspect in the area of human
simulator fidelity. The finding is of very low safety significance because the
  performance associated with resources in that the licensee did not provide
discrepancy did not have an adverse impact on operator actions such that safety
  operators with adequate facilities and equipment for use in operator training
related equipment was made inoperable during normal operations or in response
  [H.2(d)]. (Section 2.6)
to a plant transient. This finding has a crosscutting aspect in the area of human
* Green. The inspectors identified a Green noncited violation of Technical
performance associated with resources in that the licensee did not provide
  Specification 5.5.1.1 involving the failure to meet procedural requirements
operators with adequate facilities and equipment for use in operator training
  governing impaired annunciators. Specifically, after the identification of a failed
[H.2(d)]. (Section 2.6)
  annunciator, operators did not enter the annunciator in the failed annunciator log
*
  or mark the affected annunciator window with an annunciator compensatory action
Green. The inspectors identified a Green noncited violation of Technical
  flag. The licensee entered this issue in their corrective action program as Action
Specification 5.5.1.1 involving the failure to meet procedural requirements
  Request AR 070700291.
governing impaired annunciators. Specifically, after the identification of a failed
  This finding was more than minor since it was associated with the human
annunciator, operators did not enter the annunciator in the failed annunciator log
  performance attribute of the initiating events cornerstone and affected the
or mark the affected annunciator window with an annunciator compensatory action
  cornerstone objective to limit the likelihood of events that upset plant stability and
flag. The licensee entered this issue in their corrective action program as Action
  challenge critical safety functions. This finding required a Phase 2 analysis in
Request AR 070700291.
  accordance with the Manual Chapter 0609, Significance Determination Process,
This finding was more than minor since it was associated with the human
  Phase 1 Worksheets since the loss of instrument air is a transient initiator resulting
performance attribute of the initiating events cornerstone and affected the
  in the loss of the feedwater system which is part of the power conversion system
cornerstone objective to limit the likelihood of events that upset plant stability and
  which can be used to mitigate the consequences of an accident. Based on the
challenge critical safety functions. This finding required a Phase 2 analysis in
  results of the Phase 2 analysis, the finding was determined to be of very low safety
accordance with the Manual Chapter 0609, Significance Determination Process,
  significance because of the low likelihood of a complete loss of instrument air and
Phase 1 Worksheets since the loss of instrument air is a transient initiator resulting
  the availability of the auxiliary feedwater system. This finding has a crosscutting
in the loss of the feedwater system which is part of the power conversion system
  aspect in the area of human performance associated with resources because the
which can be used to mitigate the consequences of an accident. Based on the
  operators were not sufficiently trained to consistently implement the annunciator
results of the Phase 2 analysis, the finding was determined to be of very low safety
  operating procedure [H.2(b)]. (Section 2.7)
significance because of the low likelihood of a complete loss of instrument air and
                                      -5-                                      Enclosure
the availability of the auxiliary feedwater system. This finding has a crosscutting
aspect in the area of human performance associated with resources because the
operators were not sufficiently trained to consistently implement the annunciator
operating procedure [H.2(b)]. (Section 2.7)


  *   Green. A Green self-revealing finding was identified associated with the failure of
Enclosure
        the reactor coolant pump controlled bleed off valve to shut during a loss of
-6-
        instrument air event. The licensee failed to adequately implement corrective
*
        actions from previously evaluated industry operating experience for new valve
Green. A Green self-revealing finding was identified associated with the failure of
        regulators that were installed in the unit. The licensee entered this issue in their
the reactor coolant pump controlled bleed off valve to shut during a loss of
        corrective action program as Action Request AR 070600873.
instrument air event. The licensee failed to adequately implement corrective
        The finding was greater than minor because it was associated with the mitigating
actions from previously evaluated industry operating experience for new valve
        systems cornerstone attribute of design control and affected the associated
regulators that were installed in the unit. The licensee entered this issue in their
        cornerstone objective to ensure the availability, reliability, and capability of systems
corrective action program as Action Request AR 070600873.
        that respond to initiating events to prevent undesirable consequences. Using
The finding was greater than minor because it was associated with the mitigating
        Manual Chapter 0609, Significance Determination Process, Phase 1 Worksheet,
systems cornerstone attribute of design control and affected the associated
        the finding is determined to have very low safety significance because the
cornerstone objective to ensure the availability, reliability, and capability of systems
        condition only affected the mitigation systems cornerstone and it was confirmed
that respond to initiating events to prevent undesirable consequences. Using
        not to result in loss of operability per Part 9900, Technical guidance, Operability
Manual Chapter 0609, Significance Determination Process, Phase 1 Worksheet,
        Determination Process for Operability and Functionality Assessment
the finding is determined to have very low safety significance because the
        (Section 2.8).
condition only affected the mitigation systems cornerstone and it was confirmed
B. Licensee-Identified Violations
not to result in loss of operability per Part 9900, Technical guidance, Operability
  None.
Determination Process for Operability and Functionality Assessment  
                                              -6-                                      Enclosure
(Section 2.8).
B.
Licensee-Identified Violations
None.


                                    REPORT DETAILS
Enclosure
1.0 SPECIAL INSPECTION SCOPE
-7-
    The NRC conducted a special inspection at San Onofre Generating Station (SONGS) to
REPORT DETAILS
    better understand the circumstances surrounding the loss of instrument air event on
1.0
    June 20, 2007. On this occasion, instrument air pressure on Unit 2 dropped significantly
SPECIAL INSPECTION SCOPE
    following the separation of a 3-inch air header in the auxiliary building. This caused the
The NRC conducted a special inspection at San Onofre Generating Station (SONGS) to
    feedwater control valves to stop functioning, resulting in an uncontrolled increase in
better understand the circumstances surrounding the loss of instrument air event on
    steam generator water level. Operators manually tripped the Unit 2 reactor. In
June 20, 2007. On this occasion, instrument air pressure on Unit 2 dropped significantly
    accordance with NRC Management Directive 8.3, it was determined that this event had
following the separation of a 3-inch air header in the auxiliary building. This caused the
    sufficient risk significance to warrant a special inspection.
feedwater control valves to stop functioning, resulting in an uncontrolled increase in
    The team used NRC Inspection Procedure 93812, Special Inspection Procedure, to
steam generator water level. Operators manually tripped the Unit 2 reactor. In
    conduct the inspection. The special inspection team reviewed procedures, corrective
accordance with NRC Management Directive 8.3, it was determined that this event had
    action documents, operator logs, design documentation, maintenance records, and
sufficient risk significance to warrant a special inspection.
    procurement records for the instrument air system. The team interviewed various
The team used NRC Inspection Procedure 93812, Special Inspection Procedure, to
    station personnel regarding the event. The team reviewed the licencees preliminary
conduct the inspection. The special inspection team reviewed procedures, corrective
    root cause analysis report, past failure records, extent of condition evaluation,
action documents, operator logs, design documentation, maintenance records, and
    immediate and long term corrective actions, and industry operating experience. A list of
procurement records for the instrument air system. The team interviewed various
    specific documents reviewed is provided in Attachment 1. The charter for the special
station personnel regarding the event. The team reviewed the licencees preliminary
    inspection is included as Attachment 2.
root cause analysis report, past failure records, extent of condition evaluation,
1.1 Event Summary
immediate and long term corrective actions, and industry operating experience. A list of
    During full power operation on June 20, 2007, a 3-inch diameter instrument air line failed
specific documents reviewed is provided in Attachment 1. The charter for the special
    at an improperly soldered joint on the Unit 2 instrument air header. The joint completely
inspection is included as Attachment 2.
    separated, resulting in a double-ended guillotine shear of the supply header and a
1.1
    complete loss of instrument air to Unit 2. The loss of instrument air pressure caused the
Event Summary
    feedwater control valves to stop functioning, and operators manually tripped the Unit 2
During full power operation on June 20, 2007, a 3-inch diameter instrument air line failed
    reactor as a result of an uncontrolled steam generator water level increase. Although
at an improperly soldered joint on the Unit 2 instrument air header. The joint completely
    instrument air is a shared system at SONGS, a backup nitrogen system can support
separated, resulting in a double-ended guillotine shear of the supply header and a
    system loads on the unaffected unit following a pipe break via excess flow check valves.
complete loss of instrument air to Unit 2. The loss of instrument air pressure caused the
    As a result, the pressure drop on Unit 3 was not as significant during the event and
feedwater control valves to stop functioning, and operators manually tripped the Unit 2
    operators maintained control of all functions.
reactor as a result of an uncontrolled steam generator water level increase. Although
    Operators located the failed piping in the Unit 2 turbine building and were able to isolate
instrument air is a shared system at SONGS, a backup nitrogen system can support
    the break approximately thirty minutes after the event began. Operators applied a
system loads on the unaffected unit following a pipe break via excess flow check valves.  
    temporary repair to the break and restored instrument air header pressure. Subsequent
As a result, the pressure drop on Unit 3 was not as significant during the event and
    investigations identified 32 additional leaking instrument air fittings in Unit 2 and Unit 3,
operators maintained control of all functions.
    possibly as a result of improper joint fabrication during initial construction. Maintenance
Operators located the failed piping in the Unit 2 turbine building and were able to isolate
    personnel placed structural clamps on the leaking fittings to prevent additional piping
the break approximately thirty minutes after the event began. Operators applied a
    separations until permanent repairs could be made.
temporary repair to the break and restored instrument air header pressure. Subsequent
    The time line below describes the major events following the separation of the
investigations identified 32 additional leaking instrument air fittings in Unit 2 and Unit 3,
    instrument air header fitting on June 20, 2007.
possibly as a result of improper joint fabrication during initial construction. Maintenance
                                              -7-                                      Enclosure
personnel placed structural clamps on the leaking fittings to prevent additional piping
separations until permanent repairs could be made.
The time line below describes the major events following the separation of the
instrument air header fitting on June 20, 2007.


Enclosure
-8-
June 20, 2007
June 20, 2007
2244 Instrument air dryer Temp/Level/DP HI alarm received.
2244
      Control room instrument air header pressure noted to be 80 psig and lowering.
Instrument air dryer Temp/Level/DP HI alarm received.
      Instrument air pressure low alarm received on Unit 2. (90 psig setpoint)
Control room instrument air header pressure noted to be 80 psig and lowering.
      Operators entered Procedure SO23-13-5, Loss of Instrument Air.
Instrument air pressure low alarm received on Unit 2. (90 psig setpoint)
2245 Unit 2 air operated valves begin to move on their own.
Operators entered Procedure SO23-13-5, Loss of Instrument Air.
      Full Flow condensate polisher demineralizer bypass valves open.
2245
      Chemical volume control system letdown flow isolates.
Unit 2 air operated valves begin to move on their own.
      Unit 3 instrument air pressure low alarm received. (90 psig setpoint)
Full Flow condensate polisher demineralizer bypass valves open.
2247 Steam Generator level noted to be 82% and rising in generator E088 on Unit 2.
Chemical volume control system letdown flow isolates.
      Operators secured charging pumps due to loss of letdown and began manually
Unit 3 instrument air pressure low alarm received. (90 psig setpoint)
      controlling pressurizer level.
2247
      Operators bypassed instrument air dryers. Indicated instrument air header
Steam Generator level noted to be 82% and rising in generator E088 on Unit 2.
      pressure in the control room increases from 42 psig to 67 psig.
Operators secured charging pumps due to loss of letdown and began manually
2248 Heater drain pump P059 trips.
controlling pressurizer level.
2250 Heater drain pump P058 trips.
Operators bypassed instrument air dryers. Indicated instrument air header  
      E088 level approaching trip set point, manually tripped the Unit 2 reactor.
pressure in the control room increases from 42 psig to 67 psig.
      Entered Procedure SO23-12-1, Standard Post Trip Actions.
2248
2252 Steam generator E088 level exceeds 100%.
Heater drain pump P059 trips.
2253 Operators manually tripped both main feed pumps.
2250
2254 Operators initiated both trains of auxiliary feedwater. (EFAS)
Heater drain pump P058 trips.
      Steam bypass control system responding sluggishly; both reactor temperature
E088 level approaching trip set point, manually tripped the Unit 2 reactor.  
      and pressure slightly higher than expected. Operators begin controlling pressure
Entered Procedure SO23-12-1, Standard Post Trip Actions.
      and temperature using one atmospheric dump valve.
2252
2258 Steam generator E088 level returns to less than 100%.
Steam generator E088 level exceeds 100%.
2303 Entered Procedure SO23-12-2, Reactor Trip Recovery.
2253
2321 Location of instrument air header rupture identified and isolated using manual
Operators manually tripped both main feed pumps.
      valves. Instrument air header pressure indicated in the control room immediately
2254
      recovers from 67 psig to 108 psig (normal operating pressure). Instrument air
Operators initiated both trains of auxiliary feedwater. (EFAS)
      dryer Temp/Level/DP HI and instrument air low pressure alarms clear.
Steam bypass control system responding sluggishly; both reactor temperature
      Temporary repair (soft patch) put in place on the instrument air header.
and pressure slightly higher than expected. Operators begin controlling pressure
2329 Component Cooling Water (CCW) Pump A noted to be in a runout condition,
and temperature using one atmospheric dump valve.
      operators started CCW Pump B.
2258
0024 NRC notified of unit trip due to uncontrolled level rise in steam generator E088
Steam generator E088 level returns to less than 100%.
      upon loss of instrument air.
2303
0030 Procedure SO23-12-1, Loss of Instrument Air, exited.
Entered Procedure SO23-12-2, Reactor Trip Recovery.
                                        -8-                                    Enclosure
2321
Location of instrument air header rupture identified and isolated using manual
valves. Instrument air header pressure indicated in the control room immediately
recovers from 67 psig to 108 psig (normal operating pressure). Instrument air
dryer Temp/Level/DP HI and instrument air low pressure alarms clear.
Temporary repair (soft patch) put in place on the instrument air header.
2329
Component Cooling Water (CCW) Pump A noted to be in a runout condition,
operators started CCW Pump B.
0024
NRC notified of unit trip due to uncontrolled level rise in steam generator E088
upon loss of instrument air.
0030
Procedure SO23-12-1, Loss of Instrument Air, exited.


1.2 Operator Response
Enclosure
    The team assessed the response of the control room operators to the loss of instrument
-9-
    air. The team reviewed operator logs, plant computer data, and strip charts to evaluate
1.2
    operator performance in coping with the event and transient; verified that operator
Operator Response
    actions were in accordance with the response required by plant procedures and training;
The team assessed the response of the control room operators to the loss of instrument
    and verified that the licensee identified and implemented appropriate corrective actions
air. The team reviewed operator logs, plant computer data, and strip charts to evaluate
    associated with personnel performance problems that occurred during the event. The
operator performance in coping with the event and transient; verified that operator
    team also conducted interviews with each of the control room operators who were on
actions were in accordance with the response required by plant procedures and training;
    shift the night of the event.
and verified that the licensee identified and implemented appropriate corrective actions
    The team concluded the operators acted appropriately to manually trip the Unit 2 reactor
associated with personnel performance problems that occurred during the event. The
    and turbine and place the unit in a safe condition. The inspectors also concluded the
team also conducted interviews with each of the control room operators who were on
    operators acted promptly and appropriately in recovering the instrument air system and
shift the night of the event.
    in maintaining Unit 3 at power. However, the team also identified several opportunities
The team concluded the operators acted appropriately to manually trip the Unit 2 reactor
    for improvement in some aspects of operator response and training associated with the
and turbine and place the unit in a safe condition. The inspectors also concluded the
    event.
operators acted promptly and appropriately in recovering the instrument air system and
    Through interviews with control room personnel, the inspectors noted a general
in maintaining Unit 3 at power. However, the team also identified several opportunities
    weakness in the operators understanding of the design and integrated operation of the
for improvement in some aspects of operator response and training associated with the
    instrument air and low pressure nitrogen systems. As an example, several operators
event.
    erroneously stated that the respiratory/service air system was supporting the Unit 3
Through interviews with control room personnel, the inspectors noted a general
    instrument air loads during the event, when in fact the Unit 3 loads were being supplied
weakness in the operators understanding of the design and integrated operation of the
    by the backup nitrogen system. Several operators also believed their efforts to bypass
instrument air and low pressure nitrogen systems. As an example, several operators
    the instrument air filters and to place an additional dryer in service had a positive effect
erroneously stated that the respiratory/service air system was supporting the Unit 3
    on restoring instrument air pressure to Unit 2, when in reality the Unit 2 instrument air
instrument air loads during the event, when in fact the Unit 3 loads were being supplied
    header pressure was not recoverable due to the complete separation of the pipe header
by the backup nitrogen system. Several operators also believed their efforts to bypass
    from the supply lines.
the instrument air filters and to place an additional dryer in service had a positive effect
    The inspectors concluded the operators understanding of the event on June 20, and
on restoring instrument air pressure to Unit 2, when in reality the Unit 2 instrument air
    their ability to diagnose and respond to future events involving a loss of instrument air,
header pressure was not recoverable due to the complete separation of the pipe header
    were complicated by the sparse control room instrumentation provided for the
from the supply lines.
    instrument air system. Specifically, operators in both control rooms are provided with
The inspectors concluded the operators understanding of the event on June 20, and
    one indication each for respiratory/service air supply pressure, backup nitrogen system
their ability to diagnose and respond to future events involving a loss of instrument air,
    supply pressure, and instrument air supply pressure. There are no indications for actual
were complicated by the sparse control room instrumentation provided for the
    air header pressure at the system loads for either Unit 2 or Unit 3. Additionally, the
instrument air system. Specifically, operators in both control rooms are provided with
    control room indications provided real-time pressure indication only; there were no strip
one indication each for respiratory/service air supply pressure, backup nitrogen system
    charts recorders to allow prompt diagnosis of pressure trends, nor were there any
supply pressure, and instrument air supply pressure. There are no indications for actual
    computer points available to provide pressure indication, tracking, or trending
air header pressure at the system loads for either Unit 2 or Unit 3. Additionally, the
    information to the control room operators.
control room indications provided real-time pressure indication only; there were no strip
    The inspectors reviewed Procedure SO23-13-5, Loss of Instrument Air, Revision 5,
charts recorders to allow prompt diagnosis of pressure trends, nor were there any
    which was the abnormal operating instruction used by the operators to respond to the
computer points available to provide pressure indication, tracking, or trending
    loss of instrument air pressure on June 20, 2007. The inspectors concluded that given
information to the control room operators.
    the limited data available to plant operators in the control rooms, the abnormal operating
The inspectors reviewed Procedure SO23-13-5, Loss of Instrument Air, Revision 5,
    instruction did not provide sufficient guidance to ensure operators would be able to take
which was the abnormal operating instruction used by the operators to respond to the
    prompt action to mitigate the effects of a loss of instrument air in all circumstances. The
loss of instrument air pressure on June 20, 2007. The inspectors concluded that given
    inspectors determined the failure to maintain an adequate operating instruction to
the limited data available to plant operators in the control rooms, the abnormal operating
    respond to a loss of instrument air was a violation of Technical Specification 5.5.1.1.
instruction did not provide sufficient guidance to ensure operators would be able to take
    This finding is described further in Section 2.5 of this report.
prompt action to mitigate the effects of a loss of instrument air in all circumstances. The
                                              -9-                                      Enclosure
inspectors determined the failure to maintain an adequate operating instruction to
respond to a loss of instrument air was a violation of Technical Specification 5.5.1.1.  
This finding is described further in Section 2.5 of this report.


    Through review of operator logs, the marked-up copy of the abnormal operating
Enclosure
    instruction for loss of instrument air used during the event, and interviews of operators,
-10-
    the inspectors identified that operators had failed to take the required actions specified
Through review of operator logs, the marked-up copy of the abnormal operating
    in the abnormal operating instruction for actuation of the backup nitrogen system.
instruction for loss of instrument air used during the event, and interviews of operators,
    Specifically, the operators did not take steps to monitor for oxygen-deficient areas of the
the inspectors identified that operators had failed to take the required actions specified
    plant caused by nitrogen leakage from the instrument air system and did not begin
in the abnormal operating instruction for actuation of the backup nitrogen system.  
    monitoring nitrogen tank levels. The inspectors also noted that control room
Specifically, the operators did not take steps to monitor for oxygen-deficient areas of the
    Annunciator 61B38, N2 SUPPLY TO INST AIR HEADER ON, failed to alarm during
plant caused by nitrogen leakage from the instrument air system and did not begin
    the event, which, when combined with the aforementioned weak operator understanding
monitoring nitrogen tank levels. The inspectors also noted that control room
    of the system and limited control room instrumentation, likely contributed to the
Annunciator 61B38, N2 SUPPLY TO INST AIR HEADER ON, failed to alarm during
    operators failure to take the actions of the abnormal operating instruction. The
the event, which, when combined with the aforementioned weak operator understanding
    inspectors noted the failure to take these actions had the potential to result in operator
of the system and limited control room instrumentation, likely contributed to the
    injury or death from entering oxygen-deficient areas in the plant. The inspectors
operators failure to take the actions of the abnormal operating instruction. The
    determined the failure to follow the requirements of the abnormal operating instruction
inspectors noted the failure to take these actions had the potential to result in operator
    was a violation of Technical Specification 5.5.1.1. This finding is discussed further in
injury or death from entering oxygen-deficient areas in the plant. The inspectors
    Section 2.2 of this report.
determined the failure to follow the requirements of the abnormal operating instruction
    The inspectors examined the post-trip review package assembled by the licensee
was a violation of Technical Specification 5.5.1.1. This finding is discussed further in
    following the trip of Unit 2. The inspectors noted the post-trip review package
Section 2.2 of this report.
    appropriately addressed the response and operation of safety-related plant equipment
The inspectors examined the post-trip review package assembled by the licensee
    to the event. The post-trip review also properly identified operator performance issues
following the trip of Unit 2. The inspectors noted the post-trip review package
    associated with a missed surveillance requirement and implemented appropriate
appropriately addressed the response and operation of safety-related plant equipment
    corrective actions. The inspectors concluded the licensees post-trip review was
to the event. The post-trip review also properly identified operator performance issues
    adequate per the guidance of Generic Letter 83-28, Required Actions Based on
associated with a missed surveillance requirement and implemented appropriate
    Generic Implications of Salem ATWS Events. However, the inspectors identified some
corrective actions. The inspectors concluded the licensees post-trip review was
    weaknesses in the scope and thoroughness of the review in regard to the nonsafety-
adequate per the guidance of Generic Letter 83-28, Required Actions Based on
    related aspects of the event. For example, the post trip review did not identify the failure
Generic Implications of Salem ATWS Events. However, the inspectors identified some
    of Annunciator 61B38 to alarm as mentioned above and described further in Section 1.4
weaknesses in the scope and thoroughness of the review in regard to the nonsafety-
    of this report. The review package also contained a typographical error identified by the
related aspects of the event. For example, the post trip review did not identify the failure
    inspectors that, had the recorded value been correct, would have indicated that the
of Annunciator 61B38 to alarm as mentioned above and described further in Section 1.4
    reactor trip circuit breakers had failed to open within their design time limit. The review
of this report. The review package also contained a typographical error identified by the
    also did not address the weaknesses in operator understanding of the event or the
inspectors that, had the recorded value been correct, would have indicated that the
    failure of operators to follow the requirements of the abnormal operating instruction for
reactor trip circuit breakers had failed to open within their design time limit. The review
    actuation of the backup nitrogen system as described above.
also did not address the weaknesses in operator understanding of the event or the
    The licensee initiated a root cause evaluation to assess the above issues related to the
failure of operators to follow the requirements of the abnormal operating instruction for
    operator response and post-trip review for the June 20, 2007, loss of instrument air
actuation of the backup nitrogen system as described above.
    event as part of Action Request AR 070700291.
The licensee initiated a root cause evaluation to assess the above issues related to the
1.3 Instrument Air System Interactions
operator response and post-trip review for the June 20, 2007, loss of instrument air
    The instrument air system at SONGS consists of three motor driven instrument air
event as part of Action Request AR 070700291.
    compressors, two parallel air dryers and four parallel air filters, all of which are located in
1.3
    the turbine building. Backup pressure sources for instrument air are provided by the low
Instrument Air System Interactions
    pressure nitrogen system and the respiratory/service air system. The instrument air
The instrument air system at SONGS consists of three motor driven instrument air
    system is designed to provide a continuous supply of filtered, dried, and essentially oil-
compressors, two parallel air dryers and four parallel air filters, all of which are located in
    free air for pneumatic instruments and valves in both units.
the turbine building. Backup pressure sources for instrument air are provided by the low
    During normal system operation, one of the compressors is in continuous operation
pressure nitrogen system and the respiratory/service air system. The instrument air
    while the other two compressors are in standby. The standby compressors will start and
system is designed to provide a continuous supply of filtered, dried, and essentially oil-
    stop automatically as required to supplement the running compressor to meet system
free air for pneumatic instruments and valves in both units.
                                              -10-                                      Enclosure
During normal system operation, one of the compressors is in continuous operation
while the other two compressors are in standby. The standby compressors will start and
stop automatically as required to supplement the running compressor to meet system


    demand. The instrument air header is divided between the two units by check valves
Enclosure
    installed in the supply headers and in the unit crossover header in the radwaste building.
-11-
    Non-safety related nitrogen supply lines with isolating valves and excess flow check
demand. The instrument air header is divided between the two units by check valves
    valves are located downstream of the unit check valves in the air supply lines to provide
installed in the supply headers and in the unit crossover header in the radwaste building.  
    a backup nitrogen supply for each units instrument air header. The excess flow check
Non-safety related nitrogen supply lines with isolating valves and excess flow check
    valves isolate on high flow, which prevents a failure in one units air piping from causing
valves are located downstream of the unit check valves in the air supply lines to provide
    an excessive instrument air pressure drop in the other unit. A second backup supply for
a backup nitrogen supply for each units instrument air header. The excess flow check
    the instrument air system is provided by the respiratory/service air system. The
valves isolate on high flow, which prevents a failure in one units air piping from causing
    respiratory/service air system is connected to the instrument air supply lines upstream of
an excessive instrument air pressure drop in the other unit. A second backup supply for
    the instrument air dryers.
the instrument air system is provided by the respiratory/service air system. The
    The instrument air system supplies the motive force to all pneumatically operated valves
respiratory/service air system is connected to the instrument air supply lines upstream of
    and instruments in both units. All pneumatically operated valves are designed to fail to
the instrument air dryers.
    their safe position on a loss of instrument air. Pneumatic valves with a safety function
The instrument air system supplies the motive force to all pneumatically operated valves
    are described in Table 9.3-1 of the SONGS Final Safety Analysis Report (FSAR) and
and instruments in both units. All pneumatically operated valves are designed to fail to
    include: saltwater cooling system isolation valves and lubrication valves, component
their safe position on a loss of instrument air. Pneumatic valves with a safety function
    cooling water isolation valves, shutdown cooling heat exchanger isolation valves, safety
are described in Table 9.3-1 of the SONGS Final Safety Analysis Report (FSAR) and
    injection line check valve leakoff line isolation valves, safety injection tank fill and drain
include: saltwater cooling system isolation valves and lubrication valves, component
    lines, and auxiliary feedwater pump steam supply valves. Significant non-safety related
cooling water isolation valves, shutdown cooling heat exchanger isolation valves, safety
    pneumatic valves include the chemical volume control system letdown isolation valves,
injection line check valve leakoff line isolation valves, safety injection tank fill and drain
    pressurizer normal spray valves, main feedwater regulating valves, steam bypass
lines, and auxiliary feedwater pump steam supply valves. Significant non-safety related
    control system valves, reactor coolant pump seal controlled bleedoff isolation valves,
pneumatic valves include the chemical volume control system letdown isolation valves,
    and component cooling water noncritical loop isolation valves.
pressurizer normal spray valves, main feedwater regulating valves, steam bypass
1.4 Plant Response
control system valves, reactor coolant pump seal controlled bleedoff isolation valves,
    The inspectors reviewed operator logs, alarm history, and available trend information to
and component cooling water noncritical loop isolation valves.
    evaluate the plant response to the loss of instrument air header pressure to ensure that
1.4
    all systems responded as designed. The inspectors concluded the instrument air
Plant Response
    system functioned as described in the FSAR. Following the break in the Unit 2 air
The inspectors reviewed operator logs, alarm history, and available trend information to
    header, the excess flow check valve in the backup nitrogen supply line to Unit 2 closed
evaluate the plant response to the loss of instrument air header pressure to ensure that
    to isolate the break and successfully mitigated the effect of the transient on Unit 3 as
all systems responded as designed. The inspectors concluded the instrument air
    designed. The inspectors also concluded the integrated plant response to the overall
system functioned as described in the FSAR. Following the break in the Unit 2 air
    transient also occurred as described in the FSAR, with some exceptions as noted below.
header, the excess flow check valve in the backup nitrogen supply line to Unit 2 closed
    In the post trip review package, the licensee noted excessive flow existed in the
to isolate the break and successfully mitigated the effect of the transient on Unit 3 as
    component cooling water (CCW) system for approximately 75 minutes following the
designed. The inspectors also concluded the integrated plant response to the overall
    event, which placed the CCW Pump A in a runout condition. The excess system flow
transient also occurred as described in the FSAR, with some exceptions as noted below.
    resulted when the shutdown cooling heat exchanger isolation valve failed open as
In the post trip review package, the licensee noted excessive flow existed in the
    designed on the loss of instrument air pressure. Although in the original plant design
component cooling water (CCW) system for approximately 75 minutes following the
    the CCW noncritical loop isolation valves failed shut on a loss of instrument air pressure
event, which placed the CCW Pump A in a runout condition. The excess system flow
    to isolate the shutdown cooling heat exchanger from the system, the licensee installed a
resulted when the shutdown cooling heat exchanger isolation valve failed open as
    modification in 1995 to allow the noncritical loop isolation valves to remain open in order
designed on the loss of instrument air pressure. Although in the original plant design
    to maintain cooling water for the reactor coolant pumps. Consequently, the opening of
the CCW noncritical loop isolation valves failed shut on a loss of instrument air pressure
    the shutdown cooling heat exchanger isolation valve placed an additional load on the
to isolate the shutdown cooling heat exchanger from the system, the licensee installed a
    system in excess of the capacity of the operating CCW pump. The inspectors
modification in 1995 to allow the noncritical loop isolation valves to remain open in order
    determined this was a violation of 10 CFR Part 50, Appendix B, Criterion III, Design
to maintain cooling water for the reactor coolant pumps. Consequently, the opening of
    Control. This finding is discussed further in Section 2.3 of this report.
the shutdown cooling heat exchanger isolation valve placed an additional load on the
    In the post-trip review package and during interviews with the inspectors, the operators
system in excess of the capacity of the operating CCW pump. The inspectors
    noted the controlled bleed off valve for the reactor coolant pump seals remained open
determined this was a violation of 10 CFR Part 50, Appendix B, Criterion III, Design
                                              -11-                                        Enclosure
Control. This finding is discussed further in Section 2.3 of this report.
In the post-trip review package and during interviews with the inspectors, the operators
noted the controlled bleed off valve for the reactor coolant pump seals remained open


    following the loss of instrument air. During interviews with the inspectors, the operators
Enclosure
    stated that in operator training in the site simulator, the CBO valve always failed shut on
-12-
    a loss of instrument air pressure, requiring the operators to trip the reactor coolant
following the loss of instrument air. During interviews with the inspectors, the operators
    pumps to ensure the integrity of the reactor coolant pump seals. As a result, when the
stated that in operator training in the site simulator, the CBO valve always failed shut on
    CBO valve indicated open during the event on June 20, 2007, control room operators
a loss of instrument air pressure, requiring the operators to trip the reactor coolant
    requested local, independent verification of the actual position of the CBO valve. The
pumps to ensure the integrity of the reactor coolant pump seals. As a result, when the
    inspectors concluded the discrepancy between actual plant response and that modeled
CBO valve indicated open during the event on June 20, 2007, control room operators
    in the simulator negatively impacted operator response to the loss of instrument air
requested local, independent verification of the actual position of the CBO valve. The
    event. The inspectors determined this simulator fidelity issue was a violation of 10 CFR
inspectors concluded the discrepancy between actual plant response and that modeled
    Part 55.46. This finding is discussed further in Section 2.6 of this report.
in the simulator negatively impacted operator response to the loss of instrument air
    In reviewing the cause for the failure of the CBO valve to close on the loss of instrument
event. The inspectors determined this simulator fidelity issue was a violation of 10 CFR
    air pressure, the licensee determined that the regulator for the valve had been replaced
Part 55.46. This finding is discussed further in Section 2.6 of this report.
    with a new style regulator in February 2004. The new style regulator was installed
In reviewing the cause for the failure of the CBO valve to close on the loss of instrument
    because the original model had become obsolete. Whereas air pressure would leak off
air pressure, the licensee determined that the regulator for the valve had been replaced
    the original model regulator causing the associated valve to close on a loss of
with a new style regulator in February 2004. The new style regulator was installed
    instrument air, the new regulator contained improved seals that locked in air pressure
because the original model had become obsolete. Whereas air pressure would leak off
    and allowed the associated valve to remain open. Although the licensees substitution
the original model regulator causing the associated valve to close on a loss of
    equivalency evaluation required a design change impact review prior to installing the
instrument air, the new regulator contained improved seals that locked in air pressure
    new model regulators in the plant, the engineers performing the impact review for the
and allowed the associated valve to remain open. Although the licensees substitution
    CBO valve failed to review the FSAR and so did not identify that the CBO valves were
equivalency evaluation required a design change impact review prior to installing the
    designed to fail closed on a loss of instrument air. A finding associated with the failure
new model regulators in the plant, the engineers performing the impact review for the
    to perform an adequate design change impact review is discussed further in Section 2.8
CBO valve failed to review the FSAR and so did not identify that the CBO valves were
    of this report.
designed to fail closed on a loss of instrument air. A finding associated with the failure
    During the loss of instrument air event, Annunciator 61B38, N2 SUPPLY TO INST AIR
to perform an adequate design change impact review is discussed further in Section 2.8
    HEADER ON, failed to alarm, complicating operating understanding of and response to
of this report.
    the event as described in Section 1.2 of this report. The licensee initiated Action
During the loss of instrument air event, Annunciator 61B38, N2 SUPPLY TO INST AIR
    Request AR 070601250 to address the failed annunciator. While in the control room
HEADER ON, failed to alarm, complicating operating understanding of and response to
    three days later, the inspectors noticed there were no labels, warning flags, or other
the event as described in Section 1.2 of this report. The licensee initiated Action
    devices affixed to or logged for the nonfunctional annunciator. The inspectors noted
Request AR 070601250 to address the failed annunciator. While in the control room
    that should a similar loss of instrument air pressure event recur, the absence of any
three days later, the inspectors noticed there were no labels, warning flags, or other
    warning labels or other devices to alert operators to the nonfunctional annunciator could
devices affixed to or logged for the nonfunctional annunciator. The inspectors noted
    cause the operators to fail to take the appropriate steps per the annunciator response
that should a similar loss of instrument air pressure event recur, the absence of any
    instruction and loss of instrument air abnormal operating instruction to monitor enclosed
warning labels or other devices to alert operators to the nonfunctional annunciator could
    spaces for oxygen concentration and monitor the nitrogen tank levels. Due to
cause the operators to fail to take the appropriate steps per the annunciator response
    instrument air system leakage, actuation of the backup nitrogen system without the
instruction and loss of instrument air abnormal operating instruction to monitor enclosed
    compensatory action of monitoring enclosed spaces for oxygen concentration could
spaces for oxygen concentration and monitor the nitrogen tank levels. Due to
    potentially result in operator injury or death from entering oxygen-deficient areas of the
instrument air system leakage, actuation of the backup nitrogen system without the
    plant. This inspectors determined the failure to appropriately track the nonfunctional
compensatory action of monitoring enclosed spaces for oxygen concentration could
    control room annunciator was a violation of Technical Specification 5.5.1.1. This finding
potentially result in operator injury or death from entering oxygen-deficient areas of the
    is discussed further in Section 2.7 of this report.
plant. This inspectors determined the failure to appropriately track the nonfunctional
1.5 Root Cause Evaluation
control room annunciator was a violation of Technical Specification 5.5.1.1. This finding
    The inspectors reviewed the accuracy and thoroughness of the licensee cause
is discussed further in Section 2.7 of this report.
    determination as described in the root cause evaluation, Unit 2 Instrument Air Soldered
1.5
    Joint Failure, performed as part of Action Request AR 070600867. The licensees root
Root Cause Evaluation
    cause evaluation used events and causal factors analysis and failure modes and effects
The inspectors reviewed the accuracy and thoroughness of the licensee cause
                                              -12-                                    Enclosure
determination as described in the root cause evaluation, Unit 2 Instrument Air Soldered
Joint Failure, performed as part of Action Request AR 070600867. The licensees root
cause evaluation used events and causal factors analysis and failure modes and effects


Enclosure
-13-
analysis to evaluate the physical piping failure, the use of operating experience at the
analysis to evaluate the physical piping failure, the use of operating experience at the
site, and the implementation of the preventive maintenance program in the instrument
site, and the implementation of the preventive maintenance program in the instrument
air system.
air system.
For the physical piping failure, the licensee performed a metallurgical analysis of the
For the physical piping failure, the licensee performed a metallurgical analysis of the
failed joint. The analysis showed the original solder coverage within the joint was less
failed joint. The analysis showed the original solder coverage within the joint was less
than 30% of the joint interface. Corrosion facilitated by residual flux in the joint
than 30% of the joint interface. Corrosion facilitated by residual flux in the joint
weakened the solder over time until the eventual failure of the fitting. The licensee
weakened the solder over time until the eventual failure of the fitting. The licensee
concluded the cause for the improper solder coverage was an improper fit up causing
concluded the cause for the improper solder coverage was an improper fit up causing
an excessive gap in the joint due to poor workmanship during initial construction. The
an excessive gap in the joint due to poor workmanship during initial construction. The
analysis concluded the cause of the poor workmanship was a lack of supervisory
analysis concluded the cause of the poor workmanship was a lack of supervisory
monitoring and reinforcement, and the root cause of the physical joint failure was a lack
monitoring and reinforcement, and the root cause of the physical joint failure was a lack
of intrusive testing and inspections of the instrument air system during initial
of intrusive testing and inspections of the instrument air system during initial
construction. The analysis did not identify corrective actions specific to the identified
construction. The analysis did not identify corrective actions specific to the identified
causes since the events examined occurred during initial construction. Corrective
causes since the events examined occurred during initial construction. Corrective
actions were identified to develop an inspection plan to locate additional leaking joints
actions were identified to develop an inspection plan to locate additional leaking joints
and to periodically inspect the clamps installed on improperly made joints until repairs
and to periodically inspect the clamps installed on improperly made joints until repairs
Line 686: Line 776:
The root cause analysis also examined the ineffective review and use of industry
The root cause analysis also examined the ineffective review and use of industry
operating experience (OE) at the site to determine why the event had not been
operating experience (OE) at the site to determine why the event had not been
prevented despite the existence of sufficient OE to foresee its occurrence. The licensee
prevented despite the existence of sufficient OE to foresee its occurrence. The licensee
concluded the ineffective use of OE was the result of an inappropriate cultural bias in
concluded the ineffective use of OE was the result of an inappropriate cultural bias in
the engineering department that led engineers to review OE from a defensive
the engineering department that led engineers to review OE from a defensive
standpoint; i.e., the goal of the engineers performing reviews was to determine why a
standpoint; i.e., the goal of the engineers performing reviews was to determine why a
particular OE was not applicable to the station. The licensee determined this culture
particular OE was not applicable to the station. The licensee determined this culture
was reinforced by insufficient site expectations for OE procedural use and
was reinforced by insufficient site expectations for OE procedural use and
documentation. The licensee developed corrective actions to strengthen site standards
documentation. The licensee developed corrective actions to strengthen site standards
and expectations for OE procedure use and documentation and to perform
and expectations for OE procedure use and documentation and to perform
benchmarking among industry peers to incorporate best practices for OE use.
benchmarking among industry peers to incorporate best practices for OE use.
The final portion of the licensees root cause evaluation examined the lack of an
The final portion of the licensees root cause evaluation examined the lack of an
adequate preventive maintenance program for the instrument air check valves and the
adequate preventive maintenance program for the instrument air check valves and the
backup nitrogen flow indication switch. The licensee concluded the apparent cause for
backup nitrogen flow indication switch. The licensee concluded the apparent cause for
the lack of preventive maintenance tasks was ineffective supervisory monitoring. The
the lack of preventive maintenance tasks was ineffective supervisory monitoring. The
licensee developed corrective actions to reinforce expectations for supervisory
licensee developed corrective actions to reinforce expectations for supervisory
performance and to implement preventive maintenance tasks for the instrument air
performance and to implement preventive maintenance tasks for the instrument air
check valves.
check valves.
The inspectors reviewed the licensees root cause evaluation and determined the
The inspectors reviewed the licensees root cause evaluation and determined the
metallurgical analysis and cause evaluation for the physical piping failure was thorough
metallurgical analysis and cause evaluation for the physical piping failure was thorough
and technically sound. However, the inspectors concluded that the root cause
and technically sound. However, the inspectors concluded that the root cause
evaluation as a whole was narrowly focused and in some cases lacked specific,
evaluation as a whole was narrowly focused and in some cases lacked specific,
comprehensive corrective actions.
comprehensive corrective actions.
The inspectors considered the evaluation to be narrowly focused since it did not fully
The inspectors considered the evaluation to be narrowly focused since it did not fully
address all the factors and behaviors that contributed to the nature, magnitude and
address all the factors and behaviors that contributed to the nature, magnitude and
timing of the event. For example, the evaluation did not discuss in detail a precursor
timing of the event. For example, the evaluation did not discuss in detail a precursor
event in the form of a failed thermowell fitting in the instrument air system that occurred
event in the form of a failed thermowell fitting in the instrument air system that occurred
in 1994. The evaluation also failed to address the poor quality of the OE review
in 1994. The evaluation also failed to address the poor quality of the OE review
performed in 1992. The extent of condition review made only a passing reference to the
performed in 1992. The extent of condition review made only a passing reference to the
                                          -13-                                      Enclosure


    domestic water system and did not contain a complete discussion of systems potentially
Enclosure
    affected by the identified root cause. Additionally, the maintenance review in the root
-14-
    cause evaluation did not discuss the scoping or performance of the instrument air
domestic water system and did not contain a complete discussion of systems potentially
    system under the Maintenance Rule (10 CFR Part 50.65). Also, the extent of cause
affected by the identified root cause. Additionally, the maintenance review in the root
    review for the failed joint noted that site engineers had not appropriately addressed the
cause evaluation did not discuss the scoping or performance of the instrument air
    instrument air system under the station Equipment Reliability Improvement Program, but
system under the Maintenance Rule (10 CFR Part 50.65). Also, the extent of cause
    the report did not appear to investigate why that had happened or whether there were
review for the failed joint noted that site engineers had not appropriately addressed the
    potentially other systems that may have been similarly overlooked.
instrument air system under the station Equipment Reliability Improvement Program, but
    The inspectors noted that the narrow focus of the report was also reflected in the
the report did not appear to investigate why that had happened or whether there were
    assignment of corrective actions. Specifically, the licensee identified poor supervisory
potentially other systems that may have been similarly overlooked.
    monitoring and oversight as an apparent cause for the improperly soldered joint, but
The inspectors noted that the narrow focus of the report was also reflected in the
    identified no corrective actions due to the age of the issue. However, later in the same
assignment of corrective actions. Specifically, the licensee identified poor supervisory
    report, the licensee identified poor supervisory monitoring and oversight as an apparent
monitoring and oversight as an apparent cause for the improperly soldered joint, but
    cause for the failure to establish adequate preventive maintenance tasks for instrument
identified no corrective actions due to the age of the issue. However, later in the same
    air system. Corrective actions in this case to reinforce standards and improve
report, the licensee identified poor supervisory monitoring and oversight as an apparent
    performance were directed only to the engineering organization.
cause for the failure to establish adequate preventive maintenance tasks for instrument
    The inspectors noted that in some cases, the causes identified in the root cause
air system. Corrective actions in this case to reinforce standards and improve
    evaluation tended to be associated with a single, broad corrective action such as
performance were directed only to the engineering organization.
    strengthen site standards. While the inspectors did not disagree with the intent of the
The inspectors noted that in some cases, the causes identified in the root cause
    corrective action, the generalized language leaves the method of implementation open
evaluation tended to be associated with a single, broad corrective action such as
    to interpretation and complicates the ability of the stations assessment organization to
strengthen site standards. While the inspectors did not disagree with the intent of the
    perform effectiveness reviews. In these cases, the inspectors concluded a set of
corrective action, the generalized language leaves the method of implementation open
    specific, focused, and measurable corrective actions may have been more appropriate.
to interpretation and complicates the ability of the stations assessment organization to
1.6 Event Precursors
perform effectiveness reviews. In these cases, the inspectors concluded a set of
    The team performed a search of corrective action program databases to identify
specific, focused, and measurable corrective actions may have been more appropriate.
    previous instrument air system piping problems that may have been precursors to the
1.6
    event on June 20, 2007. The inspectors identified the potential event precursors
Event Precursors
    described below.
The team performed a search of corrective action program databases to identify
    The inspectors noted that in June 1994, both Units 2 and 3 experienced a loss of
previous instrument air system piping problems that may have been precursors to the
    instrument air event due to the failure of a soldered joint retaining a threaded thermowell
event on June 20, 2007. The inspectors identified the potential event precursors
    attachment to the instrument air header. In the failure analysis for the fitting, the
described below.
    licensee determined the cause of the separation was poor quality workmanship that
The inspectors noted that in June 1994, both Units 2 and 3 experienced a loss of
    occurred during original installation. The licensee determined that when the fitting was
instrument air event due to the failure of a soldered joint retaining a threaded thermowell
    initially installed, it was not centered, causing an excessive gap on one side of the joint
attachment to the instrument air header. In the failure analysis for the fitting, the
    and resulting in inadequate solder penetration. The licensee also identified that the joint
licensee determined the cause of the separation was poor quality workmanship that
    was designed to be silver brazed per the manufacturers specification and should not
occurred during original installation. The licensee determined that when the fitting was
    have been soldered, and that this joint had most likely been leaking since original
initially installed, it was not centered, causing an excessive gap on one side of the joint
    installation since a portion of the pipe joint had no filler metal in it. Although this event
and resulting in inadequate solder penetration. The licensee also identified that the joint
    did not result in a reactor trip, the inspectors noted the cause and nature of the failure
was designed to be silver brazed per the manufacturers specification and should not
    were nearly identical to that experienced on June 20, 2007.
have been soldered, and that this joint had most likely been leaking since original
    In April, 2007, both Unit 2 and Unit 3 experienced a loss of instrument air event due to a
installation since a portion of the pipe joint had no filler metal in it. Although this event
    trip of the running air compressors. During this event as well as during the June 1994
did not result in a reactor trip, the inspectors noted the cause and nature of the failure
    loss of instrument air event described above, the annunciator for actuation of the
were nearly identical to that experienced on June 20, 2007.
    backup nitrogen supply to the instrument air system failed to alarm in the control room.
In April, 2007, both Unit 2 and Unit 3 experienced a loss of instrument air event due to a
    Following the annunciator failure in 1994, licensee maintenance technicians noted that
trip of the running air compressors. During this event as well as during the June 1994
                                              -14-                                      Enclosure
loss of instrument air event described above, the annunciator for actuation of the
backup nitrogen supply to the instrument air system failed to alarm in the control room.  
Following the annunciator failure in 1994, licensee maintenance technicians noted that


    the limit switch was dirty. Since a replacement limit switch was not available, the
Enclosure
    technicians cleaned the installed limit switch and returned it to service. In April 2007,
-15-
    licensee maintenance technicians noted that the travel on the switch was satisfactory
the limit switch was dirty. Since a replacement limit switch was not available, the
    and there were no problems on the electrical part of the system. No other work was
technicians cleaned the installed limit switch and returned it to service. In April 2007,
    documented. During the event on June 20, 2007, the annunciator for actuation of the
licensee maintenance technicians noted that the travel on the switch was satisfactory
    backup nitrogen system again failed to alarm in the control room. Although the
and there were no problems on the electrical part of the system. No other work was
    April 2007 event was caused by a compressor failure and did not result in a reactor trip,
documented. During the event on June 20, 2007, the annunciator for actuation of the
    the inspectors noted the plant response, particularly as it related to the flow switch for
backup nitrogen system again failed to alarm in the control room. Although the
    actuation of the backup nitrogen system, was similar to the event on June 20, 2007. A
April 2007 event was caused by a compressor failure and did not result in a reactor trip,
    finding associated with the failure of the licensee to take effective corrective actions for
the inspectors noted the plant response, particularly as it related to the flow switch for
    the nitrogen system flow switch is described in Section 2.4 of this report.
actuation of the backup nitrogen system, was similar to the event on June 20, 2007. A
1.7 Instrument Air System Maintenance and Testing
finding associated with the failure of the licensee to take effective corrective actions for
    The inspectors reviewed the licensees program for maintenance and inspection of the
the nitrogen system flow switch is described in Section 2.4 of this report.
    instrument air system, particularly as it related to the historical health of the instrument
1.7
    air compressors and piping system.
Instrument Air System Maintenance and Testing
    The inspectors noted the performance of the instrument air system was monitored
The inspectors reviewed the licensees program for maintenance and inspection of the
    under performance criteria established per the guidance for Category a(2) systems
instrument air system, particularly as it related to the historical health of the instrument
    under the Maintenance Rule. During discussions with the system engineer and site
air compressors and piping system.
    Maintenance Rule coordinator, the inspectors learned the system was under
The inspectors noted the performance of the instrument air system was monitored
    consideration for goal setting and monitoring per Category a(1) of the Maintenance
under performance criteria established per the guidance for Category a(2) systems
    Rule. The licensee subsequently established goals and began monitoring the
under the Maintenance Rule. During discussions with the system engineer and site
    performance of the instrument air system per Category a(1). The team considered this
Maintenance Rule coordinator, the inspectors learned the system was under
    action appropriate. The team also noted there had been several functional failures of
consideration for goal setting and monitoring per Category a(1) of the Maintenance
    the three instrument air compressors over the past two years, and at one point earlier in
Rule. The licensee subsequently established goals and began monitoring the
    the year a temporary air compressor was installed to supplement the existing instrument
performance of the instrument air system per Category a(1). The team considered this
    air compressors. The team noted this situation was nearly identical to that described in
action appropriate. The team also noted there had been several functional failures of
    NRC Inspection Report 50-361:362/97-22 as indicative of poor performance requiring
the three instrument air compressors over the past two years, and at one point earlier in
    the goal setting and monitoring per Category a(1) of the Maintenance Rule. Given this
the year a temporary air compressor was installed to supplement the existing instrument
    operating history, the team concluded it may have been appropriate for the station to
air compressors. The team noted this situation was nearly identical to that described in
    have classified the instrument air system as Category a(1) much earlier in the year.
NRC Inspection Report 50-361:362/97-22 as indicative of poor performance requiring
    However, the inspectors noted that such classification would have had no impact on the
the goal setting and monitoring per Category a(1) of the Maintenance Rule. Given this
    prevention or mitigation of the loss of instrument air event experienced at the station on
operating history, the team concluded it may have been appropriate for the station to
    June 20, 2007.
have classified the instrument air system as Category a(1) much earlier in the year.  
    The inspectors also examined maintenance work orders for individual components in the
However, the inspectors noted that such classification would have had no impact on the
    instrument air and low pressure nitrogen systems. The inspectors noted that no
prevention or mitigation of the loss of instrument air event experienced at the station on
    preventive maintenance actions existed for the excess flow check valves in the supply
June 20, 2007.
    header for backup nitrogen to the instrument air system. The inspectors considered this
The inspectors also examined maintenance work orders for individual components in the
    inappropriate given these valves have a function credited in the FSAR to prevent a
instrument air and low pressure nitrogen systems. The inspectors noted that no
    break in one units instrument air header from causing a loss of instrument air to the
preventive maintenance actions existed for the excess flow check valves in the supply
    other unit. Since check valves can not be considered inherently reliable components,
header for backup nitrogen to the instrument air system. The inspectors considered this
    the inspectors concluded the licensee had failed to perform adequate preventive
inappropriate given these valves have a function credited in the FSAR to prevent a
    maintenance to ensure the excess flow check valves would perform their intended
break in one units instrument air header from causing a loss of instrument air to the
    function. The inspectors determined this was a violation of 10 CFR Part 50.65a(2).
other unit. Since check valves can not be considered inherently reliable components,
    However, since the excess flow check valves did perform their intended function during
the inspectors concluded the licensee had failed to perform adequate preventive
    the actual loss of instrument air event on June 20, 2007, the inspectors considered this
maintenance to ensure the excess flow check valves would perform their intended
                                            -15-                                        Enclosure
function. The inspectors determined this was a violation of 10 CFR Part 50.65a(2).  
However, since the excess flow check valves did perform their intended function during
the actual loss of instrument air event on June 20, 2007, the inspectors considered this


    violation to be minor. The licensee entered this violation in their corrective action
Enclosure
    program as Action Requests AR 070600867 and AR 070900333, and evaluated the lack
-16-
    of preventive maintenance items in the instrument air system as part of the root cause
violation to be minor. The licensee entered this violation in their corrective action
    evaluation for the loss of instrument air event.
program as Action Requests AR 070600867 and AR 070900333, and evaluated the lack
1.8 Industry Operating Experience (OE) and Potential Generic Issues
of preventive maintenance items in the instrument air system as part of the root cause
    The inspectors performed searches of operating experience databases and other
evaluation for the loss of instrument air event.
    sources to identify reports of similar problems, both inside and outside the nuclear
1.8
    industry.
Industry Operating Experience (OE) and Potential Generic Issues
    During the late 1980s and early 1990s, a significant amount of Operating
The inspectors performed searches of operating experience databases and other
    Experience (OE) identified instances where facilities had experienced transients and/or
sources to identify reports of similar problems, both inside and outside the nuclear
    trips due to failures of soldered joints in instrument air system piping due to poor
industry.
    workmanship during initial construction. The licensee documented their review of the
During the late 1980s and early 1990s, a significant amount of Operating
    industry OE in their corrective action program (CAP) as Independent Safety
Experience (OE) identified instances where facilities had experienced transients and/or
    Engineering Group Operating Experience Evaluation, dated January 22, 1992. In this
trips due to failures of soldered joints in instrument air system piping due to poor
    review, the licensee evaluated the identified causes and corrective actions from the OE
workmanship during initial construction. The licensee documented their review of the
    and determined that soldering at SONGS was loosely controlled and better training was
industry OE in their corrective action program (CAP) as Independent Safety
    necessary for welders at the facility. However, the licensee asserted in their evaluation
Engineering Group Operating Experience Evaluation, dated January 22, 1992. In this
    that failures due to inadequate fit-up or solder penetration typically occur within a
review, the licensee evaluated the identified causes and corrective actions from the OE
    relatively short time frame after startup. The licensee concluded that since the
and determined that soldering at SONGS was loosely controlled and better training was
    instrument air system had been in service for many years at SONGS and no significant
necessary for welders at the facility. However, the licensee asserted in their evaluation
    problems had yet been identified, then no corrective actions were necessary with
that failures due to inadequate fit-up or solder penetration typically occur within a
    respect to the installed instrument configuration. The inspectors considered this
relatively short time frame after startup. The licensee concluded that since the
    conclusion to be without a valid technical basis. A finding associated with this evaluation
instrument air system had been in service for many years at SONGS and no significant
    is discussed in Section 2.1 of this report.
problems had yet been identified, then no corrective actions were necessary with
    In addition to the internal site experience described above and in Section 1.6 of this
respect to the installed instrument configuration. The inspectors considered this
    report, the inspectors identified additional OE in the form of Licensee Event Reports
conclusion to be without a valid technical basis. A finding associated with this evaluation
    (LERs). Most notably, the inspectors reviewed LER 05000336/2006-002-00, Manual
is discussed in Section 2.1 of this report.
    Reactor Trip Due to Trip of Both Feed Pumps Following a Loss of Instrument Air,
In addition to the internal site experience described above and in Section 1.6 of this  
    April 21, 2006, and LER 05000440/2006-005-00, Decreasing Instrument Air Pressure
report, the inspectors identified additional OE in the form of Licensee Event Reports
    Results in Manual Reactor Protection System Actuation, February 9, 2007. Both
(LERs). Most notably, the inspectors reviewed LER 05000336/2006-002-00, Manual
    reports describe reactor trips brought about by instrument air header joint separation. In
Reactor Trip Due to Trip of Both Feed Pumps Following a Loss of Instrument Air,
    both cases, the cause of the header joint separation was inadequate workmanship
April 21, 2006, and LER 05000440/2006-005-00, Decreasing Instrument Air Pressure
    during initial construction. Though the site OE coordinator indicated the licensee
Results in Manual Reactor Protection System Actuation, February 9, 2007. Both
    reviewed all Licensee Event Reports for applicability to SONGS, the inspectors did not
reports describe reactor trips brought about by instrument air header joint separation. In
    identify any documents in the licensees corrective action program that evaluated these
both cases, the cause of the header joint separation was inadequate workmanship
    events. The inspectors determined the lack of documentation in the CAP indicated the
during initial construction. Though the site OE coordinator indicated the licensee
    site OE organization had determined the above described events were not applicable to
reviewed all Licensee Event Reports for applicability to SONGS, the inspectors did not
    SONGS. The inspectors concluded the licensee had missed multiple opportunities both
identify any documents in the licensees corrective action program that evaluated these
    historically and recently to identify the vulnerability presented by improperly made joints
events. The inspectors determined the lack of documentation in the CAP indicated the
    in the instrument air system.
site OE organization had determined the above described events were not applicable to
    Given the failure history described above, the inspectors concluded the construction
SONGS. The inspectors concluded the licensee had missed multiple opportunities both
    methods and controls in place during initial construction at SONGS were not unique.
historically and recently to identify the vulnerability presented by improperly made joints
    Therefore, the potential for separation of instrument air piping due to improperly made
in the instrument air system.
    joints represents a potential generic concern for all facilities with instrument air systems
Given the failure history described above, the inspectors concluded the construction
    utilizing soldered joints in copper piping headers.
methods and controls in place during initial construction at SONGS were not unique.  
                                              -16-                                      Enclosure
Therefore, the potential for separation of instrument air piping due to improperly made
joints represents a potential generic concern for all facilities with instrument air systems
utilizing soldered joints in copper piping headers.


2.0 SPECIAL INSPECTION FINDINGS
Enclosure
2.1 Ineffective Corrective Actions for Instrument Air Header Ruptures
-17-
    The inspectors reviewed a self-revealing Green finding involving ineffective corrective
2.0
    actions taken in response to site and industry operating experience with instrument air
SPECIAL INSPECTION FINDINGS
    header ruptures. Specifically, contrary to Section 6.2.3 of Procedure SO-123-I-1.42,
2.1
    Maintenance Division Experience Report, Revision 0, the licensee failed to implement
Ineffective Corrective Actions for Instrument Air Header Ruptures
    corrective actions to prevent recurrence for an equipment failure with the potential to
The inspectors reviewed a self-revealing Green finding involving ineffective corrective
    cause a significant plant transient, and failed to appropriately consider previous industry
actions taken in response to site and industry operating experience with instrument air
    and plant experience similar to the event. Additionally, licensee personnel failed to
header ruptures. Specifically, contrary to Section 6.2.3 of Procedure SO-123-I-1.42,
    properly evaluate and take corrective actions based on industry operating experience
Maintenance Division Experience Report, Revision 0, the licensee failed to implement
    through 2006 involving improperly made soldered joints in instrument air systems. As a
corrective actions to prevent recurrence for an equipment failure with the potential to
    result, an additional failure of an improperly made instrument air header joint occurred at
cause a significant plant transient, and failed to appropriately consider previous industry
    SONGS on June 20, 2007.
and plant experience similar to the event. Additionally, licensee personnel failed to
    On June 20, 2007, both Units 2 and 3 experienced a loss of instrument air event due to
properly evaluate and take corrective actions based on industry operating experience
    the failure of a three-inch instrument air line header fitting. As a result of the break
through 2006 involving improperly made soldered joints in instrument air systems. As a
    location, a loss of manual feedwater control occurred on Unit 2 which ultimately resulted
result, an additional failure of an improperly made instrument air header joint occurred at
    in a manual reactor trip due to high steam generator level.
SONGS on June 20, 2007.
    The licensee performed a Root Cause Evaluation of this event, as documented in Action
On June 20, 2007, both Units 2 and 3 experienced a loss of instrument air event due to
    Request AR 070600867. The licensee also performed a metallurgical analysis of the
the failure of a three-inch instrument air line header fitting. As a result of the break
    failed joint as documented in SONGS Unit 2 Instrument Air System Failed Fitting
location, a loss of manual feedwater control occurred on Unit 2 which ultimately resulted
    Metallurgical Evaluation, dated June 27, 2007. During these evaluations, the licensee
in a manual reactor trip due to high steam generator level.
    determined the root cause of the event to be poor workmanship of the header joint
The licensee performed a Root Cause Evaluation of this event, as documented in Action
    during initial installation. The licensees metallurgical analysis also concluded the fitting
Request AR 070600867. The licensee also performed a metallurgical analysis of the
    had only thirty percent solder coverage within the joint and had likely been leaking air
failed joint as documented in SONGS Unit 2 Instrument Air System Failed Fitting
    since the plants first operating cycle. Subsequent investigations by the licensee
Metallurgical Evaluation, dated June 27, 2007. During these evaluations, the licensee
    identified 32 additional joints leaking air in the instrument air headers of both units. The
determined the root cause of the event to be poor workmanship of the header joint
    licensee installed temporary structural clamps on the leaking fittings tp prevent
during initial installation. The licensees metallurgical analysis also concluded the fitting
    additional separations until permanent repairs could be made.
had only thirty percent solder coverage within the joint and had likely been leaking air
    The inspectors reviewed the licensees root cause evaluation and metallurgical analysis
since the plants first operating cycle. Subsequent investigations by the licensee
    for this event. During their review of the issue, the inspectors noted that there had been
identified 32 additional joints leaking air in the instrument air headers of both units. The
    a previous similar air header failure at SONGS, and that the licensee had previously
licensee installed temporary structural clamps on the leaking fittings tp prevent
    evaluated related industry Operating Experience (OE) involving issues with soldered
additional separations until permanent repairs could be made.
    joints.
The inspectors reviewed the licensees root cause evaluation and metallurgical analysis
    During the late 1980s and early 1990s, a significant amount of Operating Experience
for this event. During their review of the issue, the inspectors noted that there had been
    (OE) identified instances where facilities had experienced transients and/or trips due to
a previous similar air header failure at SONGS, and that the licensee had previously
    failures of soldered joints in instrument air system piping. The identified failures were
evaluated related industry Operating Experience (OE) involving issues with soldered
    due to a lack of adequate controls during the initial makeup of soldered joints.
joints.  
    Specifically, inadequate fit-up of the joints or inadequate solder penetration were
During the late 1980s and early 1990s, a significant amount of Operating Experience
    identified as the causes of the failures. The licensee performed a review documented in
(OE) identified instances where facilities had experienced transients and/or trips due to
    Independent Safety Engineering Group Operating Experience Evaluation, dated
failures of soldered joints in instrument air system piping. The identified failures were
    January 22, 1992, to evaluate applicability of the OE to the facility. In this review, the
due to a lack of adequate controls during the initial makeup of soldered joints.  
    licensee evaluated the identified causes and corrective actions from the OE and
Specifically, inadequate fit-up of the joints or inadequate solder penetration were
    determined that soldering at SONGS was loosely controlled and better training was
identified as the causes of the failures. The licensee performed a review documented in
    necessary for welders at the facility. However, the licensee asserted in the evaluation
Independent Safety Engineering Group Operating Experience Evaluation, dated
    that any failures due to inadequate fit-up or solder penetration would typically have
January 22, 1992, to evaluate applicability of the OE to the facility. In this review, the
                                              -17-                                      Enclosure
licensee evaluated the identified causes and corrective actions from the OE and
determined that soldering at SONGS was loosely controlled and better training was
necessary for welders at the facility. However, the licensee asserted in the evaluation
that any failures due to inadequate fit-up or solder penetration would typically have


    occurred within a relatively short time frame after startup. The licensee concluded that
Enclosure
    since the instrument air system had been in service for many years and no significant
-18-
    problems had yet been identified, then no corrective actions were necessary with
occurred within a relatively short time frame after startup. The licensee concluded that
    respect to the installed instrument air configuration.
since the instrument air system had been in service for many years and no significant
    In June 1994, both Units 2 and 3 experienced a loss of instrument air event. The
problems had yet been identified, then no corrective actions were necessary with
    licensee investigated the cause and determined it was due to the failure of a soldered
respect to the installed instrument air configuration.
    joint retaining a threaded attachment, a Brazolet fitting, to the air header. The Brazolet
In June 1994, both Units 2 and 3 experienced a loss of instrument air event. The
    fitting was being used for a thermowell in the instrument air header. The licensee
licensee investigated the cause and determined it was due to the failure of a soldered
    performed a failure analysis of the fitting documented in Failure Analysis Report
joint retaining a threaded attachment, a Brazolet fitting, to the air header. The Brazolet
    No. 94-006, dated July 8, 1994, to determine the cause of the joint failure. During this
fitting was being used for a thermowell in the instrument air header. The licensee
    analysis, the licensee determined the cause of the soldered fitting failure was poor
performed a failure analysis of the fitting documented in Failure Analysis Report  
    quality workmanship that occurred during original installation. The licensee determined
No. 94-006, dated July 8, 1994, to determine the cause of the joint failure. During this
    that when the fitting was initially installed, it was not centered, but rather cocked to one
analysis, the licensee determined the cause of the soldered fitting failure was poor
    side. This was not as required by the procedure and resulted in an excessive gap on
quality workmanship that occurred during original installation. The licensee determined
    one side of the joint. This gap deprived one side of the joint of filler material, resulting in
that when the fitting was initially installed, it was not centered, but rather cocked to one
    inadequate solder penetration. The licensee also identified that the joint was designed
side. This was not as required by the procedure and resulted in an excessive gap on
    to be silver brazed per the manufacturers specification and should not have been
one side of the joint. This gap deprived one side of the joint of filler material, resulting in
    soldered.
inadequate solder penetration. The licensee also identified that the joint was designed
    Based on the metallurgical analysis, the licensee determined that the joint failure in
to be silver brazed per the manufacturers specification and should not have been
    July 1994 was due to fatigue cracking that originated at the area between the soldered
soldered.
    and un-soldered sections of the joint. The failure analysis also identified that this joint
Based on the metallurgical analysis, the licensee determined that the joint failure in
    had most likely been leaking since installation. This was based on the fact that a portion
July 1994 was due to fatigue cracking that originated at the area between the soldered
    of the pipe joint had no filler metal in it. Since the joint was located approximately ten
and un-soldered sections of the joint. The failure analysis also identified that this joint
    feet off the floor in a high noise area, the leakage had not been previously identified.
had most likely been leaking since installation. This was based on the fact that a portion
    The failure analysis also recommended that to prevent recurrence, all brazolet fittings in
of the pipe joint had no filler metal in it. Since the joint was located approximately ten
    the instrument air system should be examined both for leaks and for use of solder. The
feet off the floor in a high noise area, the leakage had not been previously identified.  
    analysis further identified that properly soldered joints fittings should be able to tolerate
The failure analysis also recommended that to prevent recurrence, all brazolet fittings in
    instrument air header pressure indefinitely; however, if leaks were found, the fittings
the instrument air system should be examined both for leaks and for use of solder. The
    should be replaced using silver braze at the earliest opportunity.
analysis further identified that properly soldered joints fittings should be able to tolerate
    The inspectors concluded the licensees evaluation of OE performed in 1992 was
instrument air header pressure indefinitely; however, if leaks were found, the fittings
    inadequate in that it improperly determined that failures due to inadequate fit-up and/or
should be replaced using silver braze at the earliest opportunity.
    inadequate solder penetration would have occurred within a relatively short time frame.
The inspectors concluded the licensees evaluation of OE performed in 1992 was
    The inspectors also determined that the licensee failed to adequately reassess this
inadequate in that it improperly determined that failures due to inadequate fit-up and/or
    position following the instrument air line joint failure in 1994. The inspectors noted that
inadequate solder penetration would have occurred within a relatively short time frame.  
    as recently as 2006, the licensee had inappropriately screened additional industry OE
The inspectors also determined that the licensee failed to adequately reassess this
    relating to the failure of inadequately made instrument air piping joints as not applicable
position following the instrument air line joint failure in 1994. The inspectors noted that
    to the station. The inspectors concluded the licensee failed to take effective corrective
as recently as 2006, the licensee had inappropriately screened additional industry OE
    actions for inadequately made joints in the instrument air system since the corrective
relating to the failure of inadequately made instrument air piping joints as not applicable
    actions for the 1994 event and in response to industry OE were narrowly focused on
to the station. The inspectors concluded the licensee failed to take effective corrective
    soldered Brazolet fittings and failed to evaluate soldered joints as a whole.
actions for inadequately made joints in the instrument air system since the corrective
    The safety significance and enforcement aspects of this finding are described in
actions for the 1994 event and in response to industry OE were narrowly focused on
    Sections 3.1 and 4.1, respectively.
soldered Brazolet fittings and failed to evaluate soldered joints as a whole.
2.2 Failure to Follow Abnormal Operating Instruction for the Loss of Instrument Air
The safety significance and enforcement aspects of this finding are described in
    The inspectors identified a Green noncited violation of Technical Specification 5.5.1.1
Sections 3.1 and 4.1, respectively.
    involving the failure to meet procedural requirements following a loss of instrument air.
2.2
                                                -18-                                    Enclosure
Failure to Follow Abnormal Operating Instruction for the Loss of Instrument Air
The inspectors identified a Green noncited violation of Technical Specification 5.5.1.1
involving the failure to meet procedural requirements following a loss of instrument air.  


    Specifically, operators failed to monitor nitrogen tank levels or take precautions for the
Enclosure
    possibility of oxygen-deficient areas in the plant following actuation of the low pressure
-19-
    backup nitrogen system.
Specifically, operators failed to monitor nitrogen tank levels or take precautions for the
    The instrument air system at SONGS utilizes a low pressure nitrogen system as a
possibility of oxygen-deficient areas in the plant following actuation of the low pressure
    backup pressure source. An instrument air system pressure drop below 83 psig will
backup nitrogen system.
    automatically actuate a control valve in the nitrogen system to supplement the
The instrument air system at SONGS utilizes a low pressure nitrogen system as a
    instrument air from liquid nitrogen storage tanks. A flow switch downstream of the
backup pressure source. An instrument air system pressure drop below 83 psig will
    control valve is designed to provide an annunciator in the control when the nitrogen
automatically actuate a control valve in the nitrogen system to supplement the
    system is actuated. While the air systems are being supplied by nitrogen, normal
instrument air from liquid nitrogen storage tanks. A flow switch downstream of the
    system leakage can result in oxygen-deficient areas in enclosed spaces of the plant,
control valve is designed to provide an annunciator in the control when the nitrogen
    and the liquid nitrogen tank levels will decrease more rapidly than usual from the
system is actuated. While the air systems are being supplied by nitrogen, normal
    addition of the instrument air loads. The nitrogen supply lines are provided with isolating
system leakage can result in oxygen-deficient areas in enclosed spaces of the plant,
    check valves and excess flow check valves to prevent a failure in one units piping from
and the liquid nitrogen tank levels will decrease more rapidly than usual from the
    causing an excessive pressure drop in the other unit.
addition of the instrument air loads. The nitrogen supply lines are provided with isolating
    On June 20, 2007, an instrument air header ruptured in Unit 2. Although the low
check valves and excess flow check valves to prevent a failure in one units piping from
    pressure nitrogen system functioned as designed to provide nitrogen to the Unit 3 air
causing an excessive pressure drop in the other unit.
    header, the control room annunciator for nitrogen system actuation did not alarm. The
On June 20, 2007, an instrument air header ruptured in Unit 2. Although the low
    instrument air header low pressure alarms did actuate on both units, and control room
pressure nitrogen system functioned as designed to provide nitrogen to the Unit 3 air
    operators began taking required actions per Procedure SO23-13-5, Loss of Instrument
header, the control room annunciator for nitrogen system actuation did not alarm. The
    Air, Revision 5. Although a step in the procedure directed operators to monitor nitrogen
instrument air header low pressure alarms did actuate on both units, and control room
    tank levels and monitor for oxygen concentrations in enclosed spaces following nitrogen
operators began taking required actions per Procedure SO23-13-5, Loss of Instrument
    system actuation, this step was not performed. The inspectors noted the failure to take
Air, Revision 5. Although a step in the procedure directed operators to monitor nitrogen
    these actions had the potential to result in a Unit 3 trip from nitrogen tank depletion or
tank levels and monitor for oxygen concentrations in enclosed spaces following nitrogen
    the injury or death of personnel from entry into oxygen-deficient spaces.
system actuation, this step was not performed. The inspectors noted the failure to take
    During interviews with the inspectors, several control room operators demonstrated
these actions had the potential to result in a Unit 3 trip from nitrogen tank depletion or
    knowledge weaknesses related to the operation of the backup pressure sources for
the injury or death of personnel from entry into oxygen-deficient spaces.
    instrument air. For example, several operators mistakenly stated the Unit 3 air header
During interviews with the inspectors, several control room operators demonstrated
    pressure had been supplied by the respiratory/service air system during the event. The
knowledge weaknesses related to the operation of the backup pressure sources for
    inspectors concluded that although the failed annunciator likely contributed to the
instrument air. For example, several operators mistakenly stated the Unit 3 air header
    operators confusion, the failure to perform the required actions of the abnormal
pressure had been supplied by the respiratory/service air system during the event. The
    operating instruction resulted from the operators poor understanding of the operation of
inspectors concluded that although the failed annunciator likely contributed to the
    the nitrogen backup to the instrument air system.
operators confusion, the failure to perform the required actions of the abnormal
    The safety significance and enforcement aspects of this finding are described in
operating instruction resulted from the operators poor understanding of the operation of
    Sections 3.2 and 4.2, respectively.
the nitrogen backup to the instrument air system.
2.3 Inadequate Evaluation Results in Runout of Component Cooling Water Pump
The safety significance and enforcement aspects of this finding are described in
    A self-revealing, Green noncited violation of 10 CFR Part 50, Appendix B, Criterion III,
Sections 3.2 and 4.2, respectively.
    Design Control, was identified when Unit 2 experienced a loss of instrument air due to
2.3
    the failure of a soldered joint. Specifically, the loss of instrument air resulted in
Inadequate Evaluation Results in Runout of Component Cooling Water Pump
    component cooling water (CCW) Pump 024 being in a runout condition for
A self-revealing, Green noncited violation of 10 CFR Part 50, Appendix B, Criterion III,
    approximately 75 minutes due to a previous system modification.
Design Control, was identified when Unit 2 experienced a loss of instrument air due to
    In 1995, the licensee implemented a design change to the CCW system to provide
the failure of a soldered joint. Specifically, the loss of instrument air resulted in
    backup nitrogen to the non-critical loop (NCL) supply and return isolation valves. The
component cooling water (CCW) Pump 024 being in a runout condition for
                                            -19-                                        Enclosure
approximately 75 minutes due to a previous system modification.  
In 1995, the licensee implemented a design change to the CCW system to provide
backup nitrogen to the non-critical loop (NCL) supply and return isolation valves. The


    design change was made to ensure that CCW flow would be maintained to the reactor
Enclosure
    coolant pump (RCP) seals during a loss of instrument air event. This would preclude
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    the licensee from the need to secure the RCPs due to a loss of CCW cooling in the
design change was made to ensure that CCW flow would be maintained to the reactor
    event of a loss of instrument air pressure.
coolant pump (RCP) seals during a loss of instrument air event. This would preclude
    On June 20, 2007, the CCW system was aligned with the Train A Pump 024 in
the licensee from the need to secure the RCPs due to a loss of CCW cooling in the
    operation with a normal full operating load on the system, including the non-critical loop.
event of a loss of instrument air pressure.
    The Train B pump was in standby. At approximately 10:45 pm, Unit 2 experienced a
On June 20, 2007, the CCW system was aligned with the Train A Pump 024 in
    loss of instrument air when a 3-inch air header fitting separated in the auxiliary building.
operation with a normal full operating load on the system, including the non-critical loop.  
    Following the loss of instrument air pressure, the shutdown cooling heat exchanger
The Train B pump was in standby. At approximately 10:45 pm, Unit 2 experienced a
    isolation valves failed opened as designed. Since the NCL isolation valves remained
loss of instrument air when a 3-inch air header fitting separated in the auxiliary building.  
    open, the increased system load from the shutdown cooling heat exchanger caused the
Following the loss of instrument air pressure, the shutdown cooling heat exchanger
    CCW pump flow rate to increase to approximately 300 gallons per minute more than its
isolation valves failed opened as designed. Since the NCL isolation valves remained
    maximum design flow limit of 16,000 gallons per minute, placing the pump in a runout
open, the increased system load from the shutdown cooling heat exchanger caused the
    condition. The pump operated in this condition for approximately 75 minutes before
CCW pump flow rate to increase to approximately 300 gallons per minute more than its
    operators took action to reduce system flow rate.
maximum design flow limit of 16,000 gallons per minute, placing the pump in a runout
    The inspectors reviewed this issue and determined that the licensee had not performed
condition. The pump operated in this condition for approximately 75 minutes before
    an adequate hydraulic analysis of the CCW system in 1995 when implementing the
operators took action to reduce system flow rate.
    design change to maintain the NCL supply and return isolation valves open following a
The inspectors reviewed this issue and determined that the licensee had not performed
    loss of instrument air. The inspectors determined that this design change directly
an adequate hydraulic analysis of the CCW system in 1995 when implementing the
    contributed to placing the CCW pump in a runout condition following the loss of
design change to maintain the NCL supply and return isolation valves open following a
    instrument air.
loss of instrument air. The inspectors determined that this design change directly
    The safety significance and enforcement aspects of this finding are described in
contributed to placing the CCW pump in a runout condition following the loss of
    Sections 3.3 and 4.3, respectively.
instrument air.
2.4 Ineffective Corrective Actions for a Failed Control Room Annunciator
The safety significance and enforcement aspects of this finding are described in
    The inspectors reviewed a self-revealing Green finding involving the failure to take
Sections 3.3 and 4.3, respectively.
    effective corrective actions for a failed control room annunciator. Specifically, after the
2.4
    annunciator for actuation of the backup nitrogen supply to the instrument air system
Ineffective Corrective Actions for a Failed Control Room Annunciator
    failed to function on demand on several occasions from 1994 through 2007, the
The inspectors reviewed a self-revealing Green finding involving the failure to take
    corrective actions taken by the licensee to restore the annunciator to service were
effective corrective actions for a failed control room annunciator. Specifically, after the
    inadequate and narrowly focused. The annunciator subsequently failed to function
annunciator for actuation of the backup nitrogen supply to the instrument air system
    during the loss of instrument air event on June 20, 2007.
failed to function on demand on several occasions from 1994 through 2007, the
    In June 1994, SONGS Units 2 and 3 experienced a loss of instrument air event during
corrective actions taken by the licensee to restore the annunciator to service were
    which the annunciator for actuation of the backup nitrogen supply to the instrument air
inadequate and narrowly focused. The annunciator subsequently failed to function
    system failed to actuate in the control room. The licensee entered this into their
during the loss of instrument air event on June 20, 2007.
    corrective action program and generated Maintenance Order 94062628000 to
In June 1994, SONGS Units 2 and 3 experienced a loss of instrument air event during
    investigate and correct the issue. During the investigation, licensee maintenance
which the annunciator for actuation of the backup nitrogen supply to the instrument air
    technicians noted that the limit switch was dirty. Since a replacement limit switch was
system failed to actuate in the control room. The licensee entered this into their
    not available, the licensee cleaned the installed limit switch and returned it to service.
corrective action program and generated Maintenance Order 94062628000 to
    The work order subsequently closed with no further actions taken by the licensee.
investigate and correct the issue. During the investigation, licensee maintenance
    While the licensee was performing an evolution to repressurize the backup nitrogen line
technicians noted that the limit switch was dirty. Since a replacement limit switch was
    to the instrument air system in May 1996, the annunciator for actuation of the backup
not available, the licensee cleaned the installed limit switch and returned it to service.  
    nitrogen supply to instrument air again failed to actuate in the control room. The
The work order subsequently closed with no further actions taken by the licensee.
    licensee entered this event into their corrective action program as Action Request
While the licensee was performing an evolution to repressurize the backup nitrogen line
    AR 960500111. In this AR the licensee determined that possible causes of the failure
to the instrument air system in May 1996, the annunciator for actuation of the backup
                                              -20-                                    Enclosure
nitrogen supply to instrument air again failed to actuate in the control room. The
licensee entered this event into their corrective action program as Action Request
AR 960500111. In this AR the licensee determined that possible causes of the failure


    were slow flow rate, not enough to flow to open the check valve far enough to trip the
Enclosure
    limit switch, or the possibility of a problem with the limit switch. The licensee generated
-21-
    Maintenance Order 94062628001 to investigate and correct the issue. During their
were slow flow rate, not enough to flow to open the check valve far enough to trip the
    inspection, the licensee maintenance technicians found rust on the limit switch and
limit switch, or the possibility of a problem with the limit switch. The licensee generated
    determined this to be the cause of the failure. The limit switch was replaced, and the
Maintenance Order 94062628001 to investigate and correct the issue. During their
    licensee verified that it worked electrically. The inspectors noted the maintenance order
inspection, the licensee maintenance technicians found rust on the limit switch and
    called for an operational test of the limit switch, but none was performed.
determined this to be the cause of the failure. The limit switch was replaced, and the
    In April 2007, Units 2 and 3 experienced a loss of instrument air event. During this
licensee verified that it worked electrically. The inspectors noted the maintenance order
    event, the annunciator for actuation of the backup nitrogen supply to the instrument air
called for an operational test of the limit switch, but none was performed.
    system again failed to actuate in the control room. The licensee entered this into their
In April 2007, Units 2 and 3 experienced a loss of instrument air event. During this
    corrective action program as AR 070400776 and generated Maintenance Order
event, the annunciator for actuation of the backup nitrogen supply to the instrument air
    07041277000 to investigate and correct the issue. During their inspection, the licensee
system again failed to actuate in the control room. The licensee entered this into their
    maintenance technicians noted that the travel on the switch was satisfactory and there
corrective action program as AR 070400776 and generated Maintenance Order
    were no problems on the electrical part of the system. No other work was documented.
07041277000 to investigate and correct the issue. During their inspection, the licensee
    On June 20, 2007, both Unit 2 and Unit 3 experienced a loss of instrument air pressure
maintenance technicians noted that the travel on the switch was satisfactory and there
    due to the failure of a three-inch instrument air line header fitting. During this event, the
were no problems on the electrical part of the system. No other work was documented.
    annunciator for actuation of the backup nitrogen supply to the instrument air system
On June 20, 2007, both Unit 2 and Unit 3 experienced a loss of instrument air pressure
    failed to actuate in the control room again. The licensee entered this into their corrective
due to the failure of a three-inch instrument air line header fitting. During this event, the
    action program as AR 070601250.
annunciator for actuation of the backup nitrogen supply to the instrument air system
    The inspectors concluded that the licensee failed to adequately evaluate and correct the
failed to actuate in the control room again. The licensee entered this into their corrective
    issue associated with the limit switch. During their review, the inspectors also noted that
action program as AR 070601250.
    the licensee had not questioned or investigated the operational aspects of the limit
The inspectors concluded that the licensee failed to adequately evaluate and correct the
    switch. Instead, the licensee had narrowly focused on testing only the electrical portion
issue associated with the limit switch. During their review, the inspectors also noted that
    of the system. The inspectors determined that the licensee had not operationally tested
the licensee had not questioned or investigated the operational aspects of the limit
    the limit switch during any of their corrective actions.
switch. Instead, the licensee had narrowly focused on testing only the electrical portion
    The licensee subsequently performed an operational test of the limit switch. During this
of the system. The inspectors determined that the licensee had not operationally tested
    testing, the licensee determined the nitrogen flow through the check valve was not
the limit switch during any of their corrective actions.
    sufficient to actuate the limit switch. Consequently, the limit switch would never have
The licensee subsequently performed an operational test of the limit switch. During this
    functioned to actuate its associated control room annunciator. The licensee entered this
testing, the licensee determined the nitrogen flow through the check valve was not
    issue into their corrective action program.
sufficient to actuate the limit switch. Consequently, the limit switch would never have
    The safety significance and enforcement aspects of this finding are described in
functioned to actuate its associated control room annunciator. The licensee entered this
    Sections 3.4 and 4.4, respectively.
issue into their corrective action program.  
2.5 Inadequate Procedure for a Loss of Instrument Air
The safety significance and enforcement aspects of this finding are described in
    The inspectors identified a Green noncited violation of Technical Specification 5.5.1.1
Sections 3.4 and 4.4, respectively.
    involving the failure to maintain an adequate abnormal operating instruction for a loss of
2.5
    instrument air event.
Inadequate Procedure for a Loss of Instrument Air
    Procedure SO23-13-5, Loss of Instrument Air, Revision 5, specifies operator actions to
The inspectors identified a Green noncited violation of Technical Specification 5.5.1.1
    mitigate the effects of excessive instrument air system leakage or the loss of the
involving the failure to maintain an adequate abnormal operating instruction for a loss of
    instrument air compressors. The inspectors reviewed the procedure and noted the
instrument air event.
    following:
Procedure SO23-13-5, Loss of Instrument Air, Revision 5, specifies operator actions to
    *       Step 1.a of the procedure was followed by a caution stating:
mitigate the effects of excessive instrument air system leakage or the loss of the
                                              -21-                                    Enclosure
instrument air compressors.   The inspectors reviewed the procedure and noted the
following:
*
Step 1.a of the procedure was followed by a caution stating:


            A large break downstream of the nitrogen supply may cause the nitrogen
Enclosure
            excess flow check valve to seat. This may be indicated by falling nitrogen
-22-
            header pressure on 2/3PI-5344B, followed by rapid return to > 80 psig.
A large break downstream of the nitrogen supply may cause the nitrogen
            The inspectors noted the nitrogen header pressure indication on 2/3PI-5344B
excess flow check valve to seat. This may be indicated by falling nitrogen
            was not provided with a strip chart recorder or computer point to provide trend
header pressure on 2/3PI-5344B, followed by rapid return to > 80 psig.
            information and the procedure did not direct stationing a dedicated operator to
The inspectors noted the nitrogen header pressure indication on 2/3PI-5344B
            monitor the pressure instruments. The inspectors concluded that absent a
was not provided with a strip chart recorder or computer point to provide trend
            dedicated operator to observe the pressure indicator, no trend information would
information and the procedure did not direct stationing a dedicated operator to
            be available to the control room operators to determine whether the described
monitor the pressure instruments. The inspectors concluded that absent a
            pressure response had occurred.
dedicated operator to observe the pressure indicator, no trend information would
    *       Step 1.b of the procedure directed operators to determine whether or not the
be available to the control room operators to determine whether the described
            instrument air header pressure was stable or rising. The inspectors concluded
pressure response had occurred.  
            this determination would be complicated by the lack of any available trend
*
            information for all of the air header pressure instruments.
Step 1.b of the procedure directed operators to determine whether or not the
    *       Step 2.a of the procedure directed operators to trip the reactors and turbines of
instrument air header pressure was stable or rising. The inspectors concluded  
            both units in the event of a loss of both instrument air header pressure and
this determination would be complicated by the lack of any available trend
            nitrogen header pressure as indicated by the control room instruments. The
information for all of the air header pressure instruments.
            inspectors noted the control room instruments only provided pressure indication
*
            for the common headers; there were no available indications for the pressure in
Step 2.a of the procedure directed operators to trip the reactors and turbines of
            the individual headers of each unit. The inspectors noted that in the event the
both units in the event of a loss of both instrument air header pressure and
            backup nitrogen system excess flow check valves either spuriously shut or failed
nitrogen header pressure as indicated by the control room instruments. The
            to open on a complete loss of instrument air, the nitrogen header pressure
inspectors noted the control room instruments only provided pressure indication
            instrument would continue to indicate sufficient pressure despite the complete
for the common headers; there were no available indications for the pressure in
            depressurization of the instrument air headers in both units. In this case,
the individual headers of each unit. The inspectors noted that in the event the
            Step 2.a would direct operators to the Subsequent Actions section of the
backup nitrogen system excess flow check valves either spuriously shut or failed
            procedure to monitor plant response instead of the more appropriate action of
to open on a complete loss of instrument air, the nitrogen header pressure
            Step 2.b to immediately trip both units.
instrument would continue to indicate sufficient pressure despite the complete
    The inspectors determined the above issues could result in a delay of necessary
depressurization of the instrument air headers in both units. In this case,
    operator response actions to mitigate the consequences of an initiating event.
Step 2.a would direct operators to the Subsequent Actions section of the
    The safety significance and enforcement aspects of this finding are described in
procedure to monitor plant response instead of the more appropriate action of
    Sections 3.5 and 4.5, respectively.
Step 2.b to immediately trip both units.
2.6 Simulator Incorrectly Modeled Plant Response to Loss of Instrument Air
The inspectors determined the above issues could result in a delay of necessary
    A self-revealing, Green noncited violation of 10 CFR Part 55.46(c)(1) was identified
operator response actions to mitigate the consequences of an initiating event.
    involving the licensees failure to incorporate a design change in modeling plant
The safety significance and enforcement aspects of this finding are described in
    response for the plant-referenced simulator. Specifically, during operator training in the
Sections 3.5 and 4.5, respectively.
    plant-referenced simulator, the controlled bleedoff valves for the reactor coolant pumps
2.6
    were modeled to fail closed on a loss of instrument air, whereas the valves in the plant
Simulator Incorrectly Modeled Plant Response to Loss of Instrument Air
    remained open during an actual loss of instrument air event on June 20, 2007.
A self-revealing, Green noncited violation of 10 CFR Part 55.46(c)(1) was identified
    The original model regulator installed on the reactor coolant pump (RCP) controlled
involving the licensees failure to incorporate a design change in modeling plant
    bleed off (CBO) Valve 2HV9218 allowed air to bleed off on a loss of instrument air,
response for the plant-referenced simulator. Specifically, during operator training in the
    enabling the valve actuator to move shut to its fail-safe position. Though not an
plant-referenced simulator, the controlled bleedoff valves for the reactor coolant pumps
    intentional design feature of the regulator, the licensee took credit for this feature to shut
were modeled to fail closed on a loss of instrument air, whereas the valves in the plant
                                              -22-                                      Enclosure
remained open during an actual loss of instrument air event on June 20, 2007.
The original model regulator installed on the reactor coolant pump (RCP) controlled
bleed off (CBO) Valve 2HV9218 allowed air to bleed off on a loss of instrument air,
enabling the valve actuator to move shut to its fail-safe position. Though not an
intentional design feature of the regulator, the licensee took credit for this feature to shut


    the RCP CBO valve during a loss of instrument air. As such, the plant-referenced
Enclosure
    simulator used for operator training modeled the valve going shut during a loss of
-23-
    instrument air event.
the RCP CBO valve during a loss of instrument air. As such, the plant-referenced
    In February 2004, the licensee replaced the existing valve regulator for the RCP CBO
simulator used for operator training modeled the valve going shut during a loss of
    valve with a new style regulator. The new regulators were used because the original
instrument air event.
    regulator was obsolete. The vendor modified the new regulators to make them leak
In February 2004, the licensee replaced the existing valve regulator for the RCP CBO
    tight, removing the unintentional bleed off characteristic. The licensee evaluated the
valve with a new style regulator. The new regulators were used because the original
    change in the new regulators and determined the new regulators to be an equivalent
regulator was obsolete. The vendor modified the new regulators to make them leak
    valve as part of Substitute Equivalency Evaluation (SEE) 020040.
tight, removing the unintentional bleed off characteristic. The licensee evaluated the
    On June 20, 2007, both Units 2 and 3 experienced a loss of instrument air event due to
change in the new regulators and determined the new regulators to be an equivalent
    the failure of a three-inch instrument air line header fitting. During this event, the RCP
valve as part of Substitute Equivalency Evaluation (SEE) 020040.  
    CBO containment isolation Valve 2HV9218 failed to go closed as the operators
On June 20, 2007, both Units 2 and 3 experienced a loss of instrument air event due to
    expected. The control room dispatched an operator at the time of the event to
the failure of a three-inch instrument air line header fitting. During this event, the RCP
    investigate and determine why the valve did not go closed. The operator noted locally
CBO containment isolation Valve 2HV9218 failed to go closed as the operators
    that the valve was open and that pressure was present on the regulator. The control
expected. The control room dispatched an operator at the time of the event to
    room subsequently dispatched another operator to independently second-check the
investigate and determine why the valve did not go closed. The operator noted locally
    position of the valves. The second operator also noted that the valve was open and that
that the valve was open and that pressure was present on the regulator. The control
    pressure was present on the regulator. The operators took no other actions at the time
room subsequently dispatched another operator to independently second-check the
    because closure of this valve could cause loss of CBO flow which would have required
position of the valves. The second operator also noted that the valve was open and that
    the RCPs to be secured.
pressure was present on the regulator. The operators took no other actions at the time
    The inspectors determined that the licensee failed to update the plant-referenced
because closure of this valve could cause loss of CBO flow which would have required
    simulator following the CBO valve regulator change. As a result, operators were trained
the RCPs to be secured.
    that the RCP CBO valves would shut during a loss of instrument air. However, during
The inspectors determined that the licensee failed to update the plant-referenced
    the actual loss of instrument air event on June 20 the CBO valve did not go shut as
simulator following the CBO valve regulator change. As a result, operators were trained
    expected which caused confusion among the operators responding to the event.
that the RCP CBO valves would shut during a loss of instrument air. However, during
    The safety significance and enforcement aspects of this finding are described in
the actual loss of instrument air event on June 20 the CBO valve did not go shut as
    Sections 3.6 and 4.6, respectively.
expected which caused confusion among the operators responding to the event.
2.7 Failure to Follow Procedure for an Impaired Annunciator
The safety significance and enforcement aspects of this finding are described in
    The inspectors identified a Green noncited violation of Technical Specification 5.5.1.1
Sections 3.6 and 4.6, respectively.
    involving the failure to meet procedural requirements governing impaired annunciators.
2.7
    Specifically, after the identification of a failed annunciator, operators did not enter the
Failure to Follow Procedure for an Impaired Annunciator
    annunciator in the failed annunciator log or mark the affected annunciator window with
The inspectors identified a Green noncited violation of Technical Specification 5.5.1.1
    an annunciator compensatory action flag.
involving the failure to meet procedural requirements governing impaired annunciators.  
    The instrument air system at SONGS utilizes a low pressure nitrogen system as a
Specifically, after the identification of a failed annunciator, operators did not enter the
    backup pressure source. An instrument air system pressure drop will automatically
annunciator in the failed annunciator log or mark the affected annunciator window with
    actuate a control valve in the nitrogen system to supplement the instrument air from
an annunciator compensatory action flag.
    liquid nitrogen storage tanks. A flow switch downstream of the control valve is designed
The instrument air system at SONGS utilizes a low pressure nitrogen system as a
    to provide an annunciator in the control when the nitrogen system is actuated. This
backup pressure source. An instrument air system pressure drop will automatically
    annunciator is used as a diagnostic aid and to determine operator actions in
actuate a control valve in the nitrogen system to supplement the instrument air from
    Procedure SO23-13-5, Loss of Instrument Air, Revision 5.
liquid nitrogen storage tanks. A flow switch downstream of the control valve is designed
    On June 20, 2007, an instrument air header rupture occurred in Unit 2. The inspectors
to provide an annunciator in the control when the nitrogen system is actuated. This
    noted that although the low pressure nitrogen system provided nitrogen to the Unit 3 air
annunciator is used as a diagnostic aid and to determine operator actions in
    header as designed, the control room annunciator for nitrogen system actuation did not
Procedure SO23-13-5, Loss of Instrument Air, Revision 5.
                                              -23-                                    Enclosure
On June 20, 2007, an instrument air header rupture occurred in Unit 2. The inspectors
noted that although the low pressure nitrogen system provided nitrogen to the Unit 3 air
header as designed, the control room annunciator for nitrogen system actuation did not


    alarm. The licensee initiated AR 070601250 on June 29, 2007 to address the failed
Enclosure
    annunciator. On July 2, the inspectors noted the failed annunciator was not included in
-24-
    the impaired annunciator log. The licensee polled two shift managers and determined
alarm. The licensee initiated AR 070601250 on June 29, 2007 to address the failed
    that one believed the annunciator should be treated as impaired and requiring
annunciator. On July 2, the inspectors noted the failed annunciator was not included in
    compensatory actions per Procedure SO23-6-29, Operation of Annunciators and
the impaired annunciator log. The licensee polled two shift managers and determined
    Indicators, Revision 15, and the other shift manager did not. The inspectors concluded
that one believed the annunciator should be treated as impaired and requiring
    the operators were not consistently implementing the portion of the procedure
compensatory actions per Procedure SO23-6-29, Operation of Annunciators and
    concerning impaired annunciators. The licensee subsequently entered the annunciator
Indicators, Revision 15, and the other shift manager did not. The inspectors concluded
    in the impaired annunciator log and took the actions specified by Procedure SO23-6-29
the operators were not consistently implementing the portion of the procedure
    for an impaired annunciator.
concerning impaired annunciators. The licensee subsequently entered the annunciator
    The safety significance and enforcement aspects of this finding are described in
in the impaired annunciator log and took the actions specified by Procedure SO23-6-29
    Sections 3.7 and 4.7, respectively.
for an impaired annunciator.
2.8 Inadequate Implementation of Corrective Actions for Air Operated Valve Regulators
The safety significance and enforcement aspects of this finding are described in
    A Green self-revealing finding was identified associated with the failure of the reactor
Sections 3.7 and 4.7, respectively.
    coolant pump controlled bleed off valve to shut during a loss of instrument air event.
2.8
    The licensee failed to adequately implement corrective actions from previously
Inadequate Implementation of Corrective Actions for Air Operated Valve Regulators
    evaluated industry operating experience for new valve regulators that were installed in
A Green self-revealing finding was identified associated with the failure of the reactor
    the unit.
coolant pump controlled bleed off valve to shut during a loss of instrument air event.  
    In July 2002, industry Operating Experience (OE) was issued which identified potentially
The licensee failed to adequately implement corrective actions from previously
    undesirable consequences due a design change to air operated valve regulators that
evaluated industry operating experience for new valve regulators that were installed in
    improved leakage characteristics of the regulators. The old model regulators allowed air
the unit.
    pressure to bleed off on a loss of instrument air, which enabled the valve actuator to
In July 2002, industry Operating Experience (OE) was issued which identified potentially
    move to its fail-safe position. This was not an intentional design feature of the regulator.
undesirable consequences due a design change to air operated valve regulators that
    The new regulators were changed to correct this unintentional bleed off and make them
improved leakage characteristics of the regulators. The old model regulators allowed air
    leak tight. The OE was issued to alert users to this change so that if a user had taken
pressure to bleed off on a loss of instrument air, which enabled the valve actuator to
    credit for this unintentional bleed off they would be aware of this change and
move to its fail-safe position. This was not an intentional design feature of the regulator.  
    appropriately address it.
The new regulators were changed to correct this unintentional bleed off and make them
    The licensee evaluated this OE and determined that it was applicable to the station.
leak tight. The OE was issued to alert users to this change so that if a user had taken
    AR 031001558 was initiated in October 2003 to provide appropriate actions to address
credit for this unintentional bleed off they would be aware of this change and
    any issues. The licensee identified that this change would not affect air operated valves
appropriately address it.  
    that have an associated positioner or controller, or valves that are configured with a
The licensee evaluated this OE and determined that it was applicable to the station.  
    solenoid valve installed between the air regulator and actuator that receives a signal to
AR 031001558 was initiated in October 2003 to provide appropriate actions to address
    vent. Valves without an associated positioner, controller, solenoid valve, or other
any issues. The licensee identified that this change would not affect air operated valves
    configuration to allow for air bleed off could be affected by use of the new regulator.
that have an associated positioner or controller, or valves that are configured with a
    During this evaluation the licensee also determined that there were not any of the new
solenoid valve installed between the air regulator and actuator that receives a signal to
    regulators in use at the facility at the time.
vent. Valves without an associated positioner, controller, solenoid valve, or other
    The licensee had already performed Substitute Equivalency Evaluations (SEE) for
configuration to allow for air bleed off could be affected by use of the new regulator.  
    replacing some of the old style regulators with the new style. Based on the results of
During this evaluation the licensee also determined that there were not any of the new
    the OE review the licensee determined that there was a need to revise the existing
regulators in use at the facility at the time.
    SEEs to require design engineering and procurement engineering to perform a design
The licensee had already performed Substitute Equivalency Evaluations (SEE) for
    change impact review to evaluate the installation configuration. The purpose of this
replacing some of the old style regulators with the new style. Based on the results of
    review was to evaluate whether a design change would be necessary prior to installation
the OE review the licensee determined that there was a need to revise the existing
    of the new style regulators.
SEEs to require design engineering and procurement engineering to perform a design
                                              -24-                                  Enclosure
change impact review to evaluate the installation configuration. The purpose of this
review was to evaluate whether a design change would be necessary prior to installation
of the new style regulators.


    In February 2004 the licensee replaced the old style regulator with a new style regulator
Enclosure
    on the reactor coolant pump (RCP) controlled bleed off (CBO) Valve 2HV9218. This
-25-
    was evaluated under SEE 020040.
In February 2004 the licensee replaced the old style regulator with a new style regulator
    On June 20, 2007 both Units 2 and 3 experienced a loss of instrument air event due to
on the reactor coolant pump (RCP) controlled bleed off (CBO) Valve 2HV9218. This
    the failure of a three-inch instrument air line header fitting. During this event, the RCP
was evaluated under SEE 020040.
    CBO containment isolation valve, 2HV9218, failed to go closed as expected. The
On June 20, 2007 both Units 2 and 3 experienced a loss of instrument air event due to
    licensee dispatched an operator at the time of the event to investigate and determine
the failure of a three-inch instrument air line header fitting. During this event, the RCP
    why the valve did not go closed. The operator noted that the valve was open and that
CBO containment isolation valve, 2HV9218, failed to go closed as expected. The
    pressure was present on the regulator. The licensee took no other actions at the time
licensee dispatched an operator at the time of the event to investigate and determine
    because closure of this valve could cause loss of CBO flow which would have required
why the valve did not go closed. The operator noted that the valve was open and that
    the RCPs to be secured.
pressure was present on the regulator. The licensee took no other actions at the time
    The licensee performed a review of this issue as documented in AR 070600873. During
because closure of this valve could cause loss of CBO flow which would have required
    this review, the licensee determined that the valve should have shut during the loss of
the RCPs to be secured.
    instrument air event and did not because of the new style regulator that had been
The licensee performed a review of this issue as documented in AR 070600873. During
    installed. The licensee also identified that the SEE appropriately identified the
this review, the licensee determined that the valve should have shut during the loss of
    requirement for design engineering and procurement engineering to perform a design
instrument air event and did not because of the new style regulator that had been
    change impact to evaluate the installation configuration. However, the action by
installed. The licensee also identified that the SEE appropriately identified the
    procurement engineering to require a design change review prior to installation of the
requirement for design engineering and procurement engineering to perform a design
    regulator failed due to a known computer software limitation, and the maintenance
change impact to evaluate the installation configuration. However, the action by
    engineering review inappropriately determined that there were no applications where the
procurement engineering to require a design change review prior to installation of the
    old regulators did not have a solenoid or bleed off device between the regulator and
regulator failed due to a known computer software limitation, and the maintenance
    solenoid. The licensee also identified that during both of these assessments, the
engineering review inappropriately determined that there were no applications where the
    engineers did not review the UFSAR or any other licensing commitments that credited
old regulators did not have a solenoid or bleed off device between the regulator and
    bleed down characteristics of the old regulators during a loss of instrument air.
solenoid. The licensee also identified that during both of these assessments, the
    The licensee also performed an extent of condition review to determine if there were any
engineers did not review the UFSAR or any other licensing commitments that credited
    other instances of these new style regulators being installed in the plant. This review
bleed down characteristics of the old regulators during a loss of instrument air.
    identified 37 instances of the new regulators being installed in the plant without
The licensee also performed an extent of condition review to determine if there were any
    performance of a design change impact review.
other instances of these new style regulators being installed in the plant. This review
    The safety significance and enforcement aspects of this finding are described in
identified 37 instances of the new regulators being installed in the plant without
    Sections 3.8 and 4.8, respectively.
performance of a design change impact review.
3.0 ASSESSMENT
The safety significance and enforcement aspects of this finding are described in
3.1 Ineffective Corrective Actions for Instrument Air Header Ruptures
Sections 3.8 and 4.8, respectively.
    The failure to take effective corrective actions in response to site and industry operating
3.0
    experience resulting in a subsequent instrument air header failure was a performance
ASSESSMENT
    deficiency. This finding was more than minor since it was associated with the
3.1
    equipment reliability attribute of the initiating events cornerstone and affected the
Ineffective Corrective Actions for Instrument Air Header Ruptures
    cornerstone objective to limit the likelihood of events that upset plant stability and
The failure to take effective corrective actions in response to site and industry operating
    challenge critical safety functions. This finding required a Phase 2 analysis per the
experience resulting in a subsequent instrument air header failure was a performance
    Manual Chapter 0609, Significance Determination Process, Phase 1 Worksheets since
deficiency. This finding was more than minor since it was associated with the
    the loss of instrument air is a transient initiator resulting in the loss of the feedwater
equipment reliability attribute of the initiating events cornerstone and affected the
    system which is part of the power conversion system which can be used to mitigate the
cornerstone objective to limit the likelihood of events that upset plant stability and
    consequences of an accident. The inspectors performed a Phase 2 analysis using
challenge critical safety functions. This finding required a Phase 2 analysis per the
    Appendix A, Technical Basis for At-Power Significance Determination Process, and the
Manual Chapter 0609, Significance Determination Process, Phase 1 Worksheets since
    Phase 2 worksheets for SONGS. The inspectors assumed that the exposure period
the loss of instrument air is a transient initiator resulting in the loss of the feedwater
                                              -25-                                      Enclosure
system which is part of the power conversion system which can be used to mitigate the
consequences of an accident. The inspectors performed a Phase 2 analysis using
Appendix A, Technical Basis for At-Power Significance Determination Process, and the
Phase 2 worksheets for SONGS. The inspectors assumed that the exposure period


    was greater than 30 days, that the performance deficiency increased the likelihood that
Enclosure
    a complete loss of instrument air would occur, and that there was no affect on mitigating
-26-
    systems other than those modeled in the risk-informed notebook. Details of the
was greater than 30 days, that the performance deficiency increased the likelihood that
    Phase 2 analysis and a subsequent Phase 3 analysis are documented in Attachment 3.
a complete loss of instrument air would occur, and that there was no affect on mitigating
    Based on the results of the Phase 3 analysis, the finding was determined to be of very
systems other than those modeled in the risk-informed notebook. Details of the
    low safety significance (Green) because of the availability of the diverse auxiliary
Phase 2 analysis and a subsequent Phase 3 analysis are documented in Attachment 3.
    feedwater system and the ability of the operators to depressurize the steam generators
Based on the results of the Phase 3 analysis, the finding was determined to be of very
    and utilize the condensate system for heat removal. These results were evaluated by a
low safety significance (Green) because of the availability of the diverse auxiliary
    senior reactor analyst. In addition, the senior reactor analyst determined the impact of
feedwater system and the ability of the operators to depressurize the steam generators
    this performance deficiency on the likelihood of the large-early release frequency.
and utilize the condensate system for heat removal. These results were evaluated by a
    These evaluations indicated that the impacts were also of very low safety significance.
senior reactor analyst. In addition, the senior reactor analyst determined the impact of
    This finding has a crosscutting aspect in the area of problem identification and
this performance deficiency on the likelihood of the large-early release frequency.  
    resolution associated with operating experience in that the licensee failed to effectively
These evaluations indicated that the impacts were also of very low safety significance.
    implement changes to station processes, procedures, and equipment in response to
This finding has a crosscutting aspect in the area of problem identification and
    operating experience involving improperly made instrument air system joints [P.2(b)].
resolution associated with operating experience in that the licensee failed to effectively
3.2 Failure to Follow Abnormal Operating Instruction for the Loss of Instrument Air
implement changes to station processes, procedures, and equipment in response to
    The failure to follow station procedures to monitor nitrogen tank levels and oxygen
operating experience involving improperly made instrument air system joints [P.2(b)].
    concentrations in enclosed rooms where operator actions may have been required was
3.2
    a performance deficiency. This finding was more than minor since it was associated
Failure to Follow Abnormal Operating Instruction for the Loss of Instrument Air
    with the human performance attribute of the initiating events cornerstone and affected
The failure to follow station procedures to monitor nitrogen tank levels and oxygen
    the cornerstone objective to limit the likelihood of events that upset plant stability and
concentrations in enclosed rooms where operator actions may have been required was
    challenge critical safety functions. This finding required a Phase 2 analysis in
a performance deficiency. This finding was more than minor since it was associated
    accordance with the Manual Chapter 0609, Significance Determination Process,
with the human performance attribute of the initiating events cornerstone and affected
    Phase 1 Worksheets since the loss of instrument air is a transient initiator resulting in
the cornerstone objective to limit the likelihood of events that upset plant stability and
    the loss of the feedwater system which is part of the power conversion system which
challenge critical safety functions. This finding required a Phase 2 analysis in
    can be used to mitigate the consequences of an accident. The inspectors performed a
accordance with the Manual Chapter 0609, Significance Determination Process,
    Phase 2 analysis using Appendix A, Technical Basis for At-Power Significance
Phase 1 Worksheets since the loss of instrument air is a transient initiator resulting in
    Determination Process, and the Phase 2 worksheets for SONGS. The inspectors
the loss of the feedwater system which is part of the power conversion system which
    assumed that the exposure period was greater than 30 days, that the performance
can be used to mitigate the consequences of an accident. The inspectors performed a
    deficiency increased the likelihood that a complete loss of instrument air would occur,
Phase 2 analysis using Appendix A, Technical Basis for At-Power Significance
    and that there was no affect on mitigating systems other than those modeled in the risk-
Determination Process, and the Phase 2 worksheets for SONGS. The inspectors
    informed notebook. Based on the results of the Phase 2 analysis, the finding was
assumed that the exposure period was greater than 30 days, that the performance
    determined to be of very low safety significance because of the low likelihood of a
deficiency increased the likelihood that a complete loss of instrument air would occur,
    complete loss of instrument air and the availability of the auxiliary feedwater system.
and that there was no affect on mitigating systems other than those modeled in the risk-
    These results were evaluated by a senior reactor analyst. In addition, the senior reactor
informed notebook. Based on the results of the Phase 2 analysis, the finding was
    analyst determined the impact of this performance deficiency on the risk of external
determined to be of very low safety significance because of the low likelihood of a
    events and on the likelihood of the large-early release frequency. These evaluations
complete loss of instrument air and the availability of the auxiliary feedwater system.  
    indicated that the impacts were also of very low safety significance.
These results were evaluated by a senior reactor analyst. In addition, the senior reactor
    The cause of this finding has a crosscutting aspect in the area of human performance
analyst determined the impact of this performance deficiency on the risk of external
    associated with resources because licensee personnel were not adequately trained on
events and on the likelihood of the large-early release frequency. These evaluations
    the operation of the low pressure nitrogen system to effectively implement the abnormal
indicated that the impacts were also of very low safety significance.
    operating instruction [H.2(b)].
The cause of this finding has a crosscutting aspect in the area of human performance
                                              -26-                                      Enclosure
associated with resources because licensee personnel were not adequately trained on
the operation of the low pressure nitrogen system to effectively implement the abnormal
operating instruction [H.2(b)].


3.3 Inadequate Evaluation Results in Runout of Component Cooling Water Pump
Enclosure
    The failure to adequately evaluate the total system hydraulic effects prior to
-27-
    implementing a design change to supply nitrogen to the NCL isolation valves was a
3.3
    performance deficiency. This finding was greater than minor because it was associated
Inadequate Evaluation Results in Runout of Component Cooling Water Pump
    with the mitigating systems cornerstone attribute of design control and affected the
The failure to adequately evaluate the total system hydraulic effects prior to
    associated cornerstone objective to ensure the availability, reliability, and capability of
implementing a design change to supply nitrogen to the NCL isolation valves was a
    systems that respond to initiating events to prevent undesirable consequences. The
performance deficiency. This finding was greater than minor because it was associated
    finding did not affect the initiating events cornerstone functions of the component
with the mitigating systems cornerstone attribute of design control and affected the
    cooling water system because the condition would only have existed given a loss of
associated cornerstone objective to ensure the availability, reliability, and capability of
    instrument air initiator had already occurred. In accordance with NRC Inspection
systems that respond to initiating events to prevent undesirable consequences. The
    Manual Chapter 0609, Appendix A, Phase 1 Worksheet, Significance Determination
finding did not affect the initiating events cornerstone functions of the component
    Process (SDP) Phase 1 Screening Worksheet for the Initiating Events, Mitigating
cooling water system because the condition would only have existed given a loss of
    Systems, and Barriers Cornerstones, this finding was determined to be of very low
instrument air initiator had already occurred. In accordance with NRC Inspection
    safety significance because the finding was a design deficiency confirmed not to result
Manual Chapter 0609, Appendix A, Phase 1 Worksheet, Significance Determination
    in a loss of operability per Part 9900, Technical Guidance, Operability Determination
Process (SDP) Phase 1 Screening Worksheet for the Initiating Events, Mitigating
    Process for Operability and Functional Assessment.
Systems, and Barriers Cornerstones, this finding was determined to be of very low
3.4 Ineffective Corrective Actions for a Failed Control Room Annunciator
safety significance because the finding was a design deficiency confirmed not to result
    The failure to perform adequate corrective actions for a failed control room annunciator
in a loss of operability per Part 9900, Technical Guidance, Operability Determination
    resulting in the failure of the annunciator to function during an actual event was a
Process for Operability and Functional Assessment.
    performance deficiency. This finding was more than minor since it was associated with
3.4
    the human performance attribute of the initiating events cornerstone and affected the
Ineffective Corrective Actions for a Failed Control Room Annunciator
    cornerstone objective to limit the likelihood of events that upset plant stability and
The failure to perform adequate corrective actions for a failed control room annunciator
    challenge critical safety functions. This finding required a Phase 2 analysis in
resulting in the failure of the annunciator to function during an actual event was a
    accordance with the Manual Chapter 0609, Significance Determination Process,
performance deficiency. This finding was more than minor since it was associated with
    Phase 1 Worksheets since the loss of instrument air is a transient initiator resulting in
the human performance attribute of the initiating events cornerstone and affected the
    the loss of the feedwater system which is part of the power conversion system which
cornerstone objective to limit the likelihood of events that upset plant stability and
    can be used to mitigate the consequences of an accident. The inspectors performed a
challenge critical safety functions. This finding required a Phase 2 analysis in
    Phase 2 analysis using Appendix A, Technical Basis for At-Power Significance
accordance with the Manual Chapter 0609, Significance Determination Process,
    Determination Process, and the Phase 2 worksheets for SONGS. The inspectors
Phase 1 Worksheets since the loss of instrument air is a transient initiator resulting in
    assumed that the exposure period was greater than 30 days, that the performance
the loss of the feedwater system which is part of the power conversion system which
    deficiency increased the likelihood that a complete loss of instrument air would occur,
can be used to mitigate the consequences of an accident. The inspectors performed a
    and that there was no affect on mitigating systems other than those modeled in the risk-
Phase 2 analysis using Appendix A, Technical Basis for At-Power Significance
    informed notebook. Based on the results of the Phase 2 analysis, the finding was
Determination Process, and the Phase 2 worksheets for SONGS. The inspectors
    determined to be of very low safety significance because of the low likelihood of a
assumed that the exposure period was greater than 30 days, that the performance
    complete loss of instrument air and the availability of the auxiliary feedwater system.
deficiency increased the likelihood that a complete loss of instrument air would occur,
    These results were evaluated by a senior reactor analyst. In addition, the senior reactor
and that there was no affect on mitigating systems other than those modeled in the risk-
    analyst determined the impact of this performance deficiency on the risk of external
informed notebook. Based on the results of the Phase 2 analysis, the finding was
    events and on the likelihood of the large-early release frequency. These evaluations
determined to be of very low safety significance because of the low likelihood of a
    indicated that the impacts were also of very low safety significance.
complete loss of instrument air and the availability of the auxiliary feedwater system.  
    This finding has a crosscutting aspect in the area of problem identification and
These results were evaluated by a senior reactor analyst. In addition, the senior reactor
    resolution associated with the corrective action program in that the licensee failed to
analyst determined the impact of this performance deficiency on the risk of external
    thoroughly evaluate the failed annunciator such that the resolution appropriately
events and on the likelihood of the large-early release frequency. These evaluations
    addressed the causes [P.2(c)].
indicated that the impacts were also of very low safety significance.
                                              -27-                                      Enclosure
This finding has a crosscutting aspect in the area of problem identification and
resolution associated with the corrective action program in that the licensee failed to
thoroughly evaluate the failed annunciator such that the resolution appropriately
addressed the causes [P.2(c)].


3.5 Inadequate Procedure for a Loss of Instrument Air
Enclosure
    The failure to provide adequate procedural guidance to immediately diagnose and
-28-
    properly respond to an initiating event was a performance deficiency. This finding was
3.5
    more than minor because it was associated with the procedure quality attribute of the
Inadequate Procedure for a Loss of Instrument Air
    mitigating systems cornerstone and affected the cornerstone objective to ensure the
The failure to provide adequate procedural guidance to immediately diagnose and
    availability, reliability and capability of systems that respond to initiating events, in that a
properly respond to an initiating event was a performance deficiency. This finding was
    less than adequate abnormal operating procedure could have prevented operators from
more than minor because it was associated with the procedure quality attribute of the
    promptly tripping the reactor, allowing conditions to continue to degrade and resulting in
mitigating systems cornerstone and affected the cornerstone objective to ensure the
    a demand on the reactor protection system. Using the Significance Determination
availability, reliability and capability of systems that respond to initiating events, in that a
    Process Phase 1 Screening Worksheet in Appendix A of Inspection Manual Chapter
less than adequate abnormal operating procedure could have prevented operators from
    0609, the inspectors determined this finding had very low safety significance because it
promptly tripping the reactor, allowing conditions to continue to degrade and resulting in
    did not result in an actual loss of safety function per Part 9900, Technical Guidance,
a demand on the reactor protection system. Using the Significance Determination
    Operability Determination Process for Operability and Functional Assessment.
Process Phase 1 Screening Worksheet in Appendix A of Inspection Manual Chapter
    This finding has a crosscutting aspect in the area of human performance associated
0609, the inspectors determined this finding had very low safety significance because it
    with resources in that the licensee failed to provide operators with complete, accurate,
did not result in an actual loss of safety function per Part 9900, Technical Guidance,
    and up-to-date procedures [H.2(c)].
Operability Determination Process for Operability and Functional Assessment.
3.6 Simulator Incorrectly Modeled Plant Response to Loss of Instrument Air
This finding has a crosscutting aspect in the area of human performance associated
    The failure to ensure that the plant-referenced simulator correctly replicated expected
with resources in that the licensee failed to provide operators with complete, accurate,
    plant response to transient conditions was a performance deficiency. This finding was
and up-to-date procedures [H.2(c)].
    greater than minor because it was associated with the mitigating systems cornerstone
3.6
    attribute of human performance and affected the associated cornerstone objective to
Simulator Incorrectly Modeled Plant Response to Loss of Instrument Air
    ensure the availability, reliability, and capability of systems that respond to initiating
The failure to ensure that the plant-referenced simulator correctly replicated expected
    events to prevent undesirable consequences. The inspectors evaluated this finding
plant response to transient conditions was a performance deficiency. This finding was
    using the Appendix I, Licensed Operator Requalification Significance Determination
greater than minor because it was associated with the mitigating systems cornerstone
    Process worksheets of Manual Chapter 0609 because the finding is a requalification
attribute of human performance and affected the associated cornerstone objective to
    training issue related to simulator fidelity. Block 12 of the Appendix I flow chart requires
ensure the availability, reliability, and capability of systems that respond to initiating
    the inspector to determine if deviations between the plant and simulator could result in
events to prevent undesirable consequences. The inspectors evaluated this finding
    negative training or could have a negative impact on operator actions. Negative
using the Appendix I, Licensed Operator Requalification Significance Determination
    Training is defined, in a later version of the standard (ANSI 3.5-1998), as training on a
Process worksheets of Manual Chapter 0609 because the finding is a requalification
    simulator whose configuration or performance leads the operator to incorrect response
training issue related to simulator fidelity. Block 12 of the Appendix I flow chart requires
    or understanding of the reference unit. The licensee has committed to this version of
the inspector to determine if deviations between the plant and simulator could result in
    the ANS/ANSI standard for its simulator testing program for the plant-referenced
negative training or could have a negative impact on operator actions. Negative
    simulator. During the event of June 20, 2007, operators were influenced by negative
Training is defined, in a later version of the standard (ANSI 3.5-1998), as training on a
    training on the simulator to question control room indications and locally independently
simulator whose configuration or performance leads the operator to incorrect response
    verify valve positions because valves in the plant failed to respond to a loss of
or understanding of the reference unit. The licensee has committed to this version of
    instrument air as modeled in the simulator. Therefore, differences between the simulator
the ANS/ANSI standard for its simulator testing program for the plant-referenced
    and plant did have a negative impact on operator actions. The finding is of very low
simulator. During the event of June 20, 2007, operators were influenced by negative
    safety significance because the discrepancy did not have an adverse impact on operator
training on the simulator to question control room indications and locally independently
    actions such that safety related equipment was made inoperable during normal
verify valve positions because valves in the plant failed to respond to a loss of
    operations or in response to a plant transient.
instrument air as modeled in the simulator. Therefore, differences between the simulator
    This finding has a crosscutting aspect in the area of human performance associated
and plant did have a negative impact on operator actions. The finding is of very low
    with resources in that the licensee did not provide operators with adequate facilities and
safety significance because the discrepancy did not have an adverse impact on operator
    equipment for use in operator training [H.2(d)].
actions such that safety related equipment was made inoperable during normal
                                                -28-                                    Enclosure
operations or in response to a plant transient.
This finding has a crosscutting aspect in the area of human performance associated
with resources in that the licensee did not provide operators with adequate facilities and
equipment for use in operator training [H.2(d)].


3.7 Failure to Follow Procedure for an Impaired Annunciator
Enclosure
    The failure to follow station procedures resulting in an untracked nonfunctional
-29-
    annunciator was a performance deficiency. This finding was more than minor since it
3.7
    was associated with the human performance attribute of the initiating events
Failure to Follow Procedure for an Impaired Annunciator
    cornerstone and affected the cornerstone objective to limit the likelihood of events that
The failure to follow station procedures resulting in an untracked nonfunctional
    upset plant stability and challenge critical safety functions. This finding required a
annunciator was a performance deficiency. This finding was more than minor since it
    Phase 2 analysis in accordance with the Manual Chapter 0609, Significance
was associated with the human performance attribute of the initiating events
    Determination Process, Phase 1 Worksheets since the loss of instrument air is a
cornerstone and affected the cornerstone objective to limit the likelihood of events that
    transient initiator resulting in the loss of the feedwater system which is part of the power
upset plant stability and challenge critical safety functions. This finding required a
    conversion system which can be used to mitigate the consequences of an accident.
Phase 2 analysis in accordance with the Manual Chapter 0609, Significance
    The inspectors performed a Phase 2 analysis using Appendix A, Technical Basis for
Determination Process, Phase 1 Worksheets since the loss of instrument air is a
    At-Power Significance Determination Process, and the Phase 2 worksheets for
transient initiator resulting in the loss of the feedwater system which is part of the power
    SONGS. The inspectors assumed that the exposure period was greater than 30 days,
conversion system which can be used to mitigate the consequences of an accident.  
    that the performance deficiency increased the likelihood that a complete loss of
The inspectors performed a Phase 2 analysis using Appendix A, Technical Basis for
    instrument air would occur, and that there was no affect on mitigating systems other
At-Power Significance Determination Process, and the Phase 2 worksheets for
    than those modeled in the risk-informed notebook. Based on the results of the Phase 2
SONGS. The inspectors assumed that the exposure period was greater than 30 days,
    analysis, the finding was determined to be of very low safety significance because of the
that the performance deficiency increased the likelihood that a complete loss of
    low likelihood of a complete loss of instrument air and the availability of the auxiliary
instrument air would occur, and that there was no affect on mitigating systems other
    feedwater system. These results were evaluated by a senior reactor analyst. In
than those modeled in the risk-informed notebook. Based on the results of the Phase 2
    addition, the senior reactor analyst determined the impact of this performance deficiency
analysis, the finding was determined to be of very low safety significance because of the
    on the risk of external events and on the likelihood of the large-early release frequency.
low likelihood of a complete loss of instrument air and the availability of the auxiliary
    These evaluations indicated that the impacts were also of very low safety significance.
feedwater system. These results were evaluated by a senior reactor analyst. In
    This finding has a crosscutting aspect in the area of human performance associated
addition, the senior reactor analyst determined the impact of this performance deficiency
    with resources because the operators were not sufficiently trained to consistently
on the risk of external events and on the likelihood of the large-early release frequency.  
    implement the annunciator operating procedure [H.2(b)].
These evaluations indicated that the impacts were also of very low safety significance.
3.8 Inadequate Implementation of Corrective Actions for Air Operated Valve Regulators
This finding has a crosscutting aspect in the area of human performance associated
    The failure to adequately implement corrective actions from industry OE to perform a
with resources because the operators were not sufficiently trained to consistently
    design change impact review was a performance deficiency. The finding was greater
implement the annunciator operating procedure [H.2(b)].
    than minor because it was associated with the mitigating systems cornerstone attribute
3.8
    of design control and affected the associated cornerstone objective to ensure the
Inadequate Implementation of Corrective Actions for Air Operated Valve Regulators
    availability, reliability, and capability of systems that respond to initiating events to
The failure to adequately implement corrective actions from industry OE to perform a
    prevent undesirable consequences. Using Manual Chapter 0609, Significance
design change impact review was a performance deficiency. The finding was greater
    Determination Process, Phase 1 Worksheet, the finding is determined to have very low
than minor because it was associated with the mitigating systems cornerstone attribute
    safety significance because the condition only affected the mitigation systems
of design control and affected the associated cornerstone objective to ensure the
    cornerstone and it was confirmed not to result in loss of operability per Part 9900,
availability, reliability, and capability of systems that respond to initiating events to
    Technical guidance, Operability Determination Process for Operability and Functionality
prevent undesirable consequences. Using Manual Chapter 0609, Significance
    Assessment.
Determination Process, Phase 1 Worksheet, the finding is determined to have very low
4.0 ENFORCEMENT
safety significance because the condition only affected the mitigation systems
4.1 Ineffective Corrective Actions for Instrument Air Header Ruptures
cornerstone and it was confirmed not to result in loss of operability per Part 9900,
    No violation of regulatory requirements occurred since the affected equipment was not
Technical guidance, Operability Determination Process for Operability and Functionality
    safety-related. This finding was entered into the licensees corrective action program as
Assessment.
    Action Request AR 070600867 and is identified as FIN 05000361;362/2007013-01,
4.0
    Ineffective Corrective Actions for Instrument Air Header Ruptures.
ENFORCEMENT
                                                -29-                                    Enclosure
4.1
Ineffective Corrective Actions for Instrument Air Header Ruptures
No violation of regulatory requirements occurred since the affected equipment was not
safety-related. This finding was entered into the licensees corrective action program as
Action Request AR 070600867 and is identified as FIN 05000361;362/2007013-01,
Ineffective Corrective Actions for Instrument Air Header Ruptures.


4.2 Failure to Follow Abnormal Operating Instruction for the Loss of Instrument Air
Enclosure
    Technical Specification 5.5.1.1 requires written procedures to be implemented as
-30-
    recommended by Regulatory Guide 1.33, Revision 2, Appendix A, February 1978.
4.2
    Section 6.b of Appendix A recommends procedures governing actions to be taken on a
Failure to Follow Abnormal Operating Instruction for the Loss of Instrument Air
    loss of instrument air. Step 3.h of Procedure SO23-13-5, Loss of Instrument Air,
Technical Specification 5.5.1.1 requires written procedures to be implemented as
    Revision 5, required notification of all building operators of the possibility of oxygen
recommended by Regulatory Guide 1.33, Revision 2, Appendix A, February 1978.  
    deficient areas, monitoring of enclosed spaces for oxygen levels prior to entry, and
Section 6.b of Appendix A recommends procedures governing actions to be taken on a
    monitoring of liquid nitrogen inventory following actuation of the backup nitrogen system
loss of instrument air. Step 3.h of Procedure SO23-13-5, Loss of Instrument Air,
    following an instrument air leak. Contrary to this requirement, operators failed to
Revision 5, required notification of all building operators of the possibility of oxygen
    implement these actions following actuation of the nitrogen system due to an instrument
deficient areas, monitoring of enclosed spaces for oxygen levels prior to entry, and
    air line break on June 20, 2007. Because this violation was of very low safety
monitoring of liquid nitrogen inventory following actuation of the backup nitrogen system
    significance and was entered in the corrective action program as Action Request
following an instrument air leak. Contrary to this requirement, operators failed to
    AR 070700291, this violation is being treated as an NCV consistent with Section VI.A.1
implement these actions following actuation of the nitrogen system due to an instrument
    of the NRC Enforcement Policy: NCV 05000361;362/2007013-02, Failure to Follow
air line break on June 20, 2007. Because this violation was of very low safety
    Abnormal Operating Instruction for the Loss of Instrument Air.
significance and was entered in the corrective action program as Action Request
4.3 Inadequate Evaluation Results in Runout of Component Cooling Water Pump
AR 070700291, this violation is being treated as an NCV consistent with Section VI.A.1
    10 CFR Part 50, Appendix B, Criterion III, Design Control, requires, in part, that
of the NRC Enforcement Policy: NCV 05000361;362/2007013-02, Failure to Follow
    measures be established to assure that applicable regulatory requirements and the
Abnormal Operating Instruction for the Loss of Instrument Air.
    design basis, as specified in the license application, are correctly translated into
4.3
    specifications, drawings, procedures, and instructions. It further states that design
Inadequate Evaluation Results in Runout of Component Cooling Water Pump
    control measures shall provide for verifying or checking the adequacy of design, such as
10 CFR Part 50, Appendix B, Criterion III, Design Control, requires, in part, that
    by the performance of design reviews, by the use of alternate or simplified calculational
measures be established to assure that applicable regulatory requirements and the
    methods, or by the performance of a suitable testing program. Contrary to the above,
design basis, as specified in the license application, are correctly translated into
    the licensee failed to verify the adequacy of the design associated with the modification
specifications, drawings, procedures, and instructions. It further states that design
    of the CCW NCL isolation valves installed in 1995. Because this finding is of very low
control measures shall provide for verifying or checking the adequacy of design, such as
    safety significance and has been entered into the corrective action program as Action
by the performance of design reviews, by the use of alternate or simplified calculational
    Requests AR 070700051 and 070600872, this violation is being treated as an NCV
methods, or by the performance of a suitable testing program. Contrary to the above,
    consistent with Section VI.A of the NRC Enforcement Policy:
the licensee failed to verify the adequacy of the design associated with the modification
    NCV 05000361;362/2007013-03, Inadequate Evaluation Results in Runout of
of the CCW NCL isolation valves installed in 1995. Because this finding is of very low
    Component Cooling Water Pump.
safety significance and has been entered into the corrective action program as Action
4.4 Ineffective Corrective Actions for a Failed Control Room Annunciator
Requests AR 070700051 and 070600872, this violation is being treated as an NCV
    No violations of NRC requirements were identified during the review of this issue
consistent with Section VI.A of the NRC Enforcement Policy:  
    because instrument air is not a safety related system. The licensee entered this issue
NCV 05000361;362/2007013-03, Inadequate Evaluation Results in Runout of
    into the corrective action program as Action Request AR 070601250:
Component Cooling Water Pump.
    FIN 05000361;362/2007013-04, Ineffective Corrective Actions for a Failed Control
4.4
    Room Annunciator.
Ineffective Corrective Actions for a Failed Control Room Annunciator
4.5 Inadequate Procedure for a Loss of Instrument Air
No violations of NRC requirements were identified during the review of this issue
    Technical Specification 5.5.1.1 requires written procedures to be implemented as
because instrument air is not a safety related system. The licensee entered this issue
    recommended by Regulatory Guide 1.33, Quality Assurance Program Requirements,
into the corrective action program as Action Request AR 070601250:  
    Revision 2, Appendix A, February 1978. Section 6.b of Appendix A of Regulatory Guide
FIN 05000361;362/2007013-04, Ineffective Corrective Actions for a Failed Control
    1.33 recommends procedures governing actions to be taken on a loss of instrument air.
Room Annunciator.
    American National Standard ANS-3.2, Administrative Controls and Quality Assurance
4.5
    for the Operational Phase of Nuclear Power Plants, February 1976, describes the
Inadequate Procedure for a Loss of Instrument Air
    requirements for the quality of the procedures specified in Regulatory Guide 1.33.
Technical Specification 5.5.1.1 requires written procedures to be implemented as
                                              -30-                                      Enclosure
recommended by Regulatory Guide 1.33, Quality Assurance Program Requirements,
Revision 2, Appendix A, February 1978. Section 6.b of Appendix A of Regulatory Guide
1.33 recommends procedures governing actions to be taken on a loss of instrument air.  
American National Standard ANS-3.2, Administrative Controls and Quality Assurance
for the Operational Phase of Nuclear Power Plants, February 1976, describes the
requirements for the quality of the procedures specified in Regulatory Guide 1.33.  


    Section 5.3.9.1(4) of Standard ANS-3.2 requires emergency procedures to specify
Enclosure
    immediate actions for operation of controls or confirmation of automatic actions that are
-31-
    required to stop the degradation of conditions and mitigate consequences. Contrary to
Section 5.3.9.1(4) of Standard ANS-3.2 requires emergency procedures to specify
    this requirement, since its release on May 4, 2006, Revision 5 of Procedure SO23-13-5,
immediate actions for operation of controls or confirmation of automatic actions that are
    Loss of Instrument Air, did not provide adequate guidance for operators to immediately
required to stop the degradation of conditions and mitigate consequences. Contrary to
    diagnose and properly respond to a complete loss of the instrument air system.
this requirement, since its release on May 4, 2006, Revision 5 of Procedure SO23-13-5,
    Because this violation was of very low safety significance and was entered in the
Loss of Instrument Air, did not provide adequate guidance for operators to immediately
    corrective action program as Action Request AR 070801151, this violation is being
diagnose and properly respond to a complete loss of the instrument air system.  
    treated as an NCV consistent with Section VI.A.1 of the NRC Enforcement Policy:
Because this violation was of very low safety significance and was entered in the
    NCV 05000361;362/2007013-05, Inadequate Procedure for Loss of Instrument Air.
corrective action program as Action Request AR 070801151, this violation is being
4.6 Simulator Incorrectly Modeled Plant Response to Loss of Instrument Air
treated as an NCV consistent with Section VI.A.1 of the NRC Enforcement Policy:
    10 CFR Part 55.46(c)(1) requires, in part, that the plant-referenced simulator must
NCV 05000361;362/2007013-05, Inadequate Procedure for Loss of Instrument Air.
    demonstrate expected plant response to transient conditions. Contrary to this
4.6
    requirement, the response modeled by the licensees simulator for the reactor coolant
Simulator Incorrectly Modeled Plant Response to Loss of Instrument Air
    pump controlled bleedoff valves did not demonstrate expected plant response to the
10 CFR Part 55.46(c)(1) requires, in part, that the plant-referenced simulator must
    June 20, 2007 loss of instrument air event. Because this violation was of very low safety
demonstrate expected plant response to transient conditions. Contrary to this
    significance and was entered in the corrective action program as Action Requests
requirement, the response modeled by the licensees simulator for the reactor coolant
    AR 070600873 and 070900160, this violation is being treated as an NCV consistent with
pump controlled bleedoff valves did not demonstrate expected plant response to the
    Section VI.A.1 of the NRC Enforcement Policy: NCV 05000361;362/2007013-06,
June 20, 2007 loss of instrument air event. Because this violation was of very low safety
    Simulator Incorrectly Modeled Plant Response to Loss of Instrument Air.
significance and was entered in the corrective action program as Action Requests
4.7 Failure to Follow Procedure for an Impaired Annunciator
AR 070600873 and 070900160, this violation is being treated as an NCV consistent with
    Technical Specification 5.5.1.1 requires written procedures to be implemented as
Section VI.A.1 of the NRC Enforcement Policy: NCV 05000361;362/2007013-06,
    recommended by Regulatory Guide 1.33, Revision 2, Appendix A, February 1978.
Simulator Incorrectly Modeled Plant Response to Loss of Instrument Air.
    Section 1.c of Appendix A recommends administrative procedures governing equipment
4.7
    control. Section 6.2.2 of Procedure SO23-6-29, Operation of Annunciators and
Failure to Follow Procedure for an Impaired Annunciator
    Indicators, Revision 15, required tracking of impaired annunciators requiring
Technical Specification 5.5.1.1 requires written procedures to be implemented as
    compensatory actions. Contrary to this requirement, operators failed to track an
recommended by Regulatory Guide 1.33, Revision 2, Appendix A, February 1978.  
    impaired annunciator from June 29 to July 2, 2007. Because this violation was of very
Section 1.c of Appendix A recommends administrative procedures governing equipment
    low safety significance and was entered in the corrective action program as Action
control. Section 6.2.2 of Procedure SO23-6-29, Operation of Annunciators and
    Request AR 070700291, this violation is being treated as an NCV consistent with
Indicators, Revision 15, required tracking of impaired annunciators requiring
    Section VI.A.1 of the NRC Enforcement Policy: NCV 05000361;362/2007013-07,
compensatory actions. Contrary to this requirement, operators failed to track an
    Failure to Follow Procedure for an Impaired Annunciator.
impaired annunciator from June 29 to July 2, 2007. Because this violation was of very
4.8 Inadequate Implementation of Corrective Actions for Air Operated Valve Regulators
low safety significance and was entered in the corrective action program as Action
    No violation of regulatory requirements occurred. This finding was entered in the
Request AR 070700291, this violation is being treated as an NCV consistent with
    licensees corrective action program as Action Request AR 070600873:
Section VI.A.1 of the NRC Enforcement Policy: NCV 05000361;362/2007013-07,
    FIN 05000361;362/2007013-07, Inadequate Implementation of Corrective Actions for
Failure to Follow Procedure for an Impaired Annunciator.
    Air Operated Valve Regulators.
4.8
                                            -31-                                    Enclosure
Inadequate Implementation of Corrective Actions for Air Operated Valve Regulators
No violation of regulatory requirements occurred. This finding was entered in the
licensees corrective action program as Action Request AR 070600873:
FIN 05000361;362/2007013-07, Inadequate Implementation of Corrective Actions for
Air Operated Valve Regulators.


Enclosure
-32-
4OA6 Meetings, Including Exit
4OA6 Meetings, Including Exit
    On July 2, 2007, and September 13, 2007, the results of this inspection were presented
On July 2, 2007, and September 13, 2007, the results of this inspection were presented
    to Dr. R. Waldo, Vice President Nuclear Generation, and other members of his staff who
to Dr. R. Waldo, Vice President Nuclear Generation, and other members of his staff who
    acknowledged the findings. Additionally on October 11, 2007, the final results of this
acknowledged the findings. Additionally on October 11, 2007, the final results of this
    inspection were presented to A. Scherer, Manager, Nuclear Regulatory Affairs, and
inspection were presented to A. Scherer, Manager, Nuclear Regulatory Affairs, and
    other members of his staff who acknowledged the findings. The inspector confirmed
other members of his staff who acknowledged the findings. The inspector confirmed
    that no proprietary material was examined during the inspection.
that no proprietary material was examined during the inspection.
ATTACHMENT 1: SUPPLEMENTAL INFORMATION
ATTACHMENT 1: SUPPLEMENTAL INFORMATION
ATTACHMENT 2: SPECIAL INSPECTION CHARTER
ATTACHMENT 2: SPECIAL INSPECTION CHARTER  
ATTACHMENT 3: SIGNIFICANCE DETERMINATION EVALUATION
ATTACHMENT 3: SIGNIFICANCE DETERMINATION EVALUATION
                                          -32-                                    Enclosure


                              SUPPLEMENTAL INFORMATION
Attachment 1
                                KEY POINTS OF CONTACT
A1-1
SUPPLEMENTAL INFORMATION
KEY POINTS OF CONTACT
Licensee Personnel
Licensee Personnel
K. Flynn, Site Operating Experience Coordinator
K. Flynn, Site Operating Experience Coordinator
Line 1,557: Line 1,700:
D. Wilcockson, Manager, Plant Operations
D. Wilcockson, Manager, Plant Operations
C. Williams, Manager, Compliance
C. Williams, Manager, Compliance
                    LIST OF ITEMS OPENED, CLOSED, AND DISCUSSED
LIST OF ITEMS OPENED, CLOSED, AND DISCUSSED
Opened and Closed
Opened and Closed
05000361;                 FIN     Ineffective Corrective Actions for Instrument Air Header
05000361;
362/2007013-01                    Ruptures
362/2007013-01
05000361;                NCV     Failure to Follow Abnormal Operating Instruction for the
FIN
362/2007013-02                    Loss of Instrument Air
Ineffective Corrective Actions for Instrument Air Header
05000361;                 NCV     Inadequate Evaluation Results in Runout of Component
Ruptures
362/2007013-03                    Cooling Water Pump
05000361;
05000361;                 FIN     Ineffective Corrective Actions for a Failed Control Room
362/2007013-02
362/2007013-04                    Annunciator
NCV
05000361;                NCV     Inadequate Procedure for a Loss of Instrument Air
Failure to Follow Abnormal Operating Instruction for the
362/2007013-05
Loss of Instrument Air
05000361;                NCV     Simulator Incorrectly Modeled Plant Response to a Loss of
05000361;
362/2007013-06                    Instrument Air
362/2007013-03
05000361;                NCV     Failure to Follow Procedure for an Impaired Annunciator
NCV
362/2007013-07
Inadequate Evaluation Results in Runout of Component
05000361;                FIN     Inadequate Implementation of Corrective Actions for Air
Cooling Water Pump
362/2007013-08                    Operated Valve Regulators
05000361;
                                              A1-1                                Attachment 1
362/2007013-04
FIN
Ineffective Corrective Actions for a Failed Control Room
Annunciator
05000361;
362/2007013-05
NCV
Inadequate Procedure for a Loss of Instrument Air
05000361;
362/2007013-06
NCV
Simulator Incorrectly Modeled Plant Response to a Loss of
Instrument Air
05000361;
362/2007013-07
NCV
Failure to Follow Procedure for an Impaired Annunciator
05000361;
362/2007013-08
FIN
Inadequate Implementation of Corrective Actions for Air
Operated Valve Regulators


                          LIST OF DOCUMENTS REVIEWED
Attachment 1
A1-2
LIST OF DOCUMENTS REVIEWED
Procedures
Procedures
        Number                                   Title                       Revision
Number
SO23-6-29             Operation of Annunciators and Indicators                 15
Title
SO23-13-5             Loss of Instrument Air                                     5
Revision
SO123-0-A8           Trip/Transient and Event Review                           1
SO23-6-29
SO23-12-1             Standard Post Trip Actions                               21
Operation of Annunciators and Indicators
SO23-12-2             Reactor Trip Recovery                                     18
15
SO23-1-1             Instrument Air System Operation                           17
SO23-13-5
SO123-XV-5.3         Maintenance Rule Program                                   9
Loss of Instrument Air
SO23-6-29             Operation of Annunciators and Indicators                 15
5
SO123-XV-50.39.1     Division Investigative Reports                             0
SO123-0-A8
SO123-I-1.42         Maintenance Division Experience Report                     0
Trip/Transient and Event Review
SO123-XV-50           Corrective Action Process                                 6
1
SO23-12-1
Standard Post Trip Actions
21
SO23-12-2
Reactor Trip Recovery
18
SO23-1-1
Instrument Air System Operation
17
SO123-XV-5.3
Maintenance Rule Program
9
SO23-6-29
Operation of Annunciators and Indicators
15
SO123-XV-50.39.1
Division Investigative Reports
0
SO123-I-1.42
Maintenance Division Experience Report
0
SO123-XV-50
Corrective Action Process
6
Action Requests
Action Requests
070400754                   060101956                     070400766
070400754
070600867                   051000080                     050600477
060101956
070600877                   050901305                     041101801
070400766
060101956                   050901037                     070600914
070600867
070600867                   070600872                     960500111
051000080
031001558                   041000977                     010601495
050600477
070600873                   041002146                     061001297
070600877
070600914                   040901643                     060101956
050901305
070500196                   070600870                     070601250
041101801
070501276                   070400776                     060200898
060101956
050901037
070600914
070600867
070600872
960500111
031001558
041000977
010601495
070600873
041002146
061001297
070600914
040901643
060101956
070500196
070600870
070601250
070501276
070400776
060200898
Work Orders/Maintenance Work Orders
Work Orders/Maintenance Work Orders
07061161000                     94062628000                     07041277000
07061161000
06012099000                    94062628001                    07061216000
06012099000
                                            A1-2                          Attachment 1
94062628000
94062628001
07041277000
07061216000


07041921000                       05061587000                     06021071000
Attachment 1
06020520000                        05061588000                     07050347000
A1-3
05111108000                        06020580000                     05061584000
07041921000
05111009000                        05111105000                     05061585000
06020520000
                                  05111106000                     05061586000
05111108000
                                  05111107000                     07061216000
05111009000
                                  07051780000                     07061324000
05061587000
                                  05061583000                     07061325000
05061588000
                                  05061589000
06020580000
                                  05061590000
05111105000
05111106000
05111107000
07051780000
05061583000
05061589000
05061590000
06021071000
07050347000
05061584000
05061585000
05061586000
07061216000
07061324000
07061325000
Drawings
Drawings
  Number                                     Title                                 Revision
Number
F-10946M       Component Cooling Water System No. 1203                             21
Title
F-10543M       Component Cooling Water System No. 1203                             15
Revision
40191A         Compressed Air System                                               15
F-10946M
40191B         Compressed Air System                                               21
Component Cooling Water System No. 1203
40191C         Compressed Air System                                               19
21
40191D         Compressed Air System                                               34
F-10543M
40191DSO3       Compressed Air System                                               19
Component Cooling Water System No. 1203
40191F         Compressed Air System                                               13
15
40191X         Compressed Air System                                                 2
40191A
40190C         Respiratory Service Air                                             22
Compressed Air System
40192A         Auxiliary Gas System                                                 20
15
40192B         Auxiliary Gas System                                                 16
40191B
40191GSO3       Instrument Air Distribution                                           7
Compressed Air System
40191E-10       Instrument Air System                                               10
21
40191G         Instrument Air Distribution                                           8
40191C
Compressed Air System
19
40191D
Compressed Air System
34
40191DSO3
Compressed Air System
19
40191F
Compressed Air System
13
40191X
Compressed Air System
2
40190C
Respiratory Service Air
22
40192A
Auxiliary Gas System
20
40192B
Auxiliary Gas System
16
40191GSO3
Instrument Air Distribution
7
40191E-10
Instrument Air System
10
40191G
Instrument Air Distribution
8
Calculations
Calculations
M-DSC-429, Evaluation of Joint Restraint Clamp on Instrument Air Piping, Revision 0
M-DSC-429, Evaluation of Joint Restraint Clamp on Instrument Air Piping, Revision 0
M-0091, Backup Nitrogen for the Instrument Air System Equipment Sizing, Revision 0
M-0091, Backup Nitrogen for the Instrument Air System Equipment Sizing, Revision 0
IPE-HC-006, Operator Action Summary Data Sheet Post-Initiator Human Error Probability
IPE-HC-006, Operator Action Summary Data Sheet Post-Initiator Human Error Probability  
      Calculation Worksheet
Calculation Worksheet
                                            A1-3                              Attachment 1


Attachment 1
A1-4
Miscellaneous Information
Miscellaneous Information
PRA-07-007, PRA Preliminary Evaluation of Loss of Instrument Air Event Resulting in Unit 2
PRA-07-007, PRA Preliminary Evaluation of Loss of Instrument Air Event Resulting in Unit 2  
        Trip, Dated June 22, 2007
Trip, Dated June 22, 2007
Operator Action Summary Data Sheet Post-Initiator Human Error Probability Calculation
Operator Action Summary Data Sheet Post-Initiator Human Error Probability Calculation  
        Worksheet
Worksheet
DBD-SO23-540, Instrument Air/Dedicated Backup Nitrogen System, Revision 6
DBD-SO23-540, Instrument Air/Dedicated Backup Nitrogen System, Revision 6
Engineering Change Package 070600914-6, Revision 0
Engineering Change Package 070600914-6, Revision 0  
SONGS 2 Instrument Air System Failed Fitting Metallurgical Evaluation
SONGS 2 Instrument Air System Failed Fitting Metallurgical Evaluation
SONGS System Health Reports for the Instrument Air System and Vendor Owned Nitrogen
SONGS System Health Reports for the Instrument Air System and Vendor Owned Nitrogen  
        Package
Package
Failure Analysis Report No. 94-006, Failure Analysis of the Instrument Air Fitting for
Failure Analysis Report No. 94-006, Failure Analysis of the Instrument Air Fitting for
        Temperature Gauge 2/3TI5380
Temperature Gauge 2/3TI5380
Failure Analysis Report No. 94-009, Failure Analysis of the Instrument Air Fitting for
Failure Analysis Report No. 94-009, Failure Analysis of the Instrument Air Fitting for
        Temperature Gauge 2/3TI5380, Supplement 1, Dated October 3, 1994
Temperature Gauge 2/3TI5380, Supplement 1, Dated October 3, 1994
DBD-SO23-540, Instrument Air/Dedicated Backup Nitrogen Systems, Revision 6
DBD-SO23-540, Instrument Air/Dedicated Backup Nitrogen Systems, Revision 6
Maintenance Rule Guide Book, Dated February 2004
Maintenance Rule Guide Book, Dated February 2004
SD-SO23-400, Component Cooling Water System, Revision 6
SD-SO23-400, Component Cooling Water System, Revision 6  
Meeting Agenda Maintenance Rule Expert Panel, Dated June 21, 2007
Meeting Agenda Maintenance Rule Expert Panel, Dated June 21, 2007
Regulatory Guide 1.160, Monitoring the Effectiveness of Maintenance at Nuclear Power Plants,
Regulatory Guide 1.160, Monitoring the Effectiveness of Maintenance at Nuclear Power Plants,  
        Revision 2
Revision 2
Licensee Event Report No. 2007-001-01, Revision 1, Dated August 24, 2004
Licensee Event Report No. 2007-001-01, Revision 1, Dated August 24, 2004  
Substitute Equivalency Evaluation 020040, Substitute 67CFR-237 Series Regulator for 67AFR-
Substitute Equivalency Evaluation 020040, Substitute 67CFR-237 Series Regulator for 67AFR-
        237, Revision 1
237, Revision 1
                                            A1-4                                    Attachment 1


                                          June 26, 2007
A2-1
Attachment 2
June 26, 2007
MEMORANDUM TO: Geoffrey Miller, Senior Resident Inspector, Grand Gulf
MEMORANDUM TO: Geoffrey Miller, Senior Resident Inspector, Grand Gulf
                      Jeffrey Josey, Resident Inspector, Arkansas Nuclear One
Jeffrey Josey, Resident Inspector, Arkansas Nuclear One
FROM:                 Arthur T. Howell III, Director, Division of Reactor Projects /RA AVegel for/
FROM:
SUBJECT:               SPECIAL INSPECTION CHARTER TO EVALUATE THE SAN ONOFRE
Arthur T. Howell III, Director, Division of Reactor Projects /RA AVegel for/
                      NUCLEAR GENERATING STATION INSTRUMENT AIR FAILURE
SUBJECT:  
SPECIAL INSPECTION CHARTER TO EVALUATE THE SAN ONOFRE
NUCLEAR GENERATING STATION INSTRUMENT AIR FAILURE
A Special Inspection Team is being chartered in response to the Unit 2 San Onofre Nuclear
A Special Inspection Team is being chartered in response to the Unit 2 San Onofre Nuclear
Generating Station loss of instrument air event on June 20, 2007. You are hereby designated
Generating Station loss of instrument air event on June 20, 2007. You are hereby designated
as the Special Inspection Team members. Mr. Miller is designated as the team leader. The
as the Special Inspection Team members. Mr. Miller is designated as the team leader. The
assigned SRA to support the team is David Loveless.
assigned SRA to support the team is David Loveless.
A.     Basis
A.
      On June 20, 2007, a 3-inch diameter instrument air line failed. At SONGS, instrument
Basis
      air is a shared system, but the system is equipped with certain protective features
On June 20, 2007, a 3-inch diameter instrument air line failed. At SONGS, instrument
      (excess flow check valves) to ensure that a failure in the piping system on one unit does
air is a shared system, but the system is equipped with certain protective features
      not significantly affect instrument air pressure on the other unit. On Unit 2, instrument
(excess flow check valves) to ensure that a failure in the piping system on one unit does
      air pressure dropped significantly, from approximately 110 psig to about 43 psig. The
not significantly affect instrument air pressure on the other unit. On Unit 2, instrument
      loss of instrument air pressure caused the feedwater control valves to stop functioning
air pressure dropped significantly, from approximately 110 psig to about 43 psig. The
      and water level in the steam generators increased in an uncontrolled manner.
loss of instrument air pressure caused the feedwater control valves to stop functioning
      Operators manually tripped the reactor. The operators also lost control of the steam
and water level in the steam generators increased in an uncontrolled manner.  
      dumps to the condenser (the normal heat removal method) and controlled steam
Operators manually tripped the reactor. The operators also lost control of the steam
      generator pressure and decay heat removal using the steam generator atmospheric
dumps to the condenser (the normal heat removal method) and controlled steam
      dump valves. The chemical and volume control system letdown function auto-isolated
generator pressure and decay heat removal using the steam generator atmospheric
      and operators manually controlled pressurizer level with a charging pump. On Unit 3,
dump valves. The chemical and volume control system letdown function auto-isolated
      the pressure drop was not as significant but appeared to be more than expected.
and operators manually controlled pressurizer level with a charging pump. On Unit 3,
      However, Unit 3 Operators maintained control of all functions during the event.
the pressure drop was not as significant but appeared to be more than expected.  
      Operators were able to isolate the failed instrument air line approximately 30 minutes
However, Unit 3 Operators maintained control of all functions during the event.  
      later and regained control of the Unit 2 condenser steam dumps.
Operators were able to isolate the failed instrument air line approximately 30 minutes
      During post-trip discussions with the operators, one operator stated that they had
later and regained control of the Unit 2 condenser steam dumps.
      experienced other instrument air piping failures but the affected piping was much
During post-trip discussions with the operators, one operator stated that they had
      smaller and did not significantly challenge plant operations. One such failure occurred
experienced other instrument air piping failures but the affected piping was much
      in 1994.
smaller and did not significantly challenge plant operations. One such failure occurred
      This Special Inspection Team is chartered to review the circumstances related to
in 1994.
      historical and present instrument air piping problems and assess the effectiveness of the
This Special Inspection Team is chartered to review the circumstances related to
                                                A2-1                                  Attachment 2
historical and present instrument air piping problems and assess the effectiveness of the


  licensees actions for resolving these problems. The team will also assess the
A2-2
  effectiveness of the immediate actions taken by the licensee in response to the loss of
Attachment 2
  instrument air event on June 20, 2007.
licensees actions for resolving these problems. The team will also assess the
B. Scope
effectiveness of the immediate actions taken by the licensee in response to the loss of
  The team is expected to address the following:
instrument air event on June 20, 2007.
  1.     Develop a chronology (time-line) that includes significant event elements.
B.
  2.     Evaluate the operator response to the event. Ensure that operators responded
Scope
          in accordance with plant procedures and took appropriate mitigating actions.
The team is expected to address the following:
  3.     Develop an understanding of the interface between instrument air and other risk
1.
          important systems, including the possible reliance, either short term or long term,
Develop a chronology (time-line) that includes significant event elements.
          of safety related components on instrument air.
2.
  4.     Evaluate the plant response to the event. Ensure that all systems responded as
Evaluate the operator response to the event. Ensure that operators responded
          designed. In particular, verify that design provisions, intended to prevent failure
in accordance with plant procedures and took appropriate mitigating actions.
          in one units piping from causing an excessive pressure drop in the other unit,
3.
          worked properly (see UFSAR Sections 9.3.1.1.E and 9.3.1.2.3).
Develop an understanding of the interface between instrument air and other risk
  5.     Assess the licensees root cause determination for the instrument air piping
important systems, including the possible reliance, either short term or long term,
          failure, the extent of condition review, the common cause evaluation and
of safety related components on instrument air.
          corrective measures. Evaluate whether the timeliness of the corrective
4.
          measures are consistent with the safety significance of the problems.
Evaluate the plant response to the event. Ensure that all systems responded as
  6.     Identify previous instrument air piping problems that may have been precursors
designed. In particular, verify that design provisions, intended to prevent failure
          to the June 20 event, including one event in 1994. Evaluate the licensees
in one units piping from causing an excessive pressure drop in the other unit,
          corrective measures and extent of condition reviews for those problems.
worked properly (see UFSAR Sections 9.3.1.1.E and 9.3.1.2.3).
  7.     Evaluate the licensees instrument air system maintenance and testing
5.
          programs. Verify that the programs are adequate and that the licensee is
Assess the licensees root cause determination for the instrument air piping
          following the program provisions. Pay particular attention to the historical health
failure, the extent of condition review, the common cause evaluation and
          of the instrument air compressors and piping system.
corrective measures. Evaluate whether the timeliness of the corrective
  8.     Evaluate pertinent industry operating experience that represent potential
measures are consistent with the safety significance of the problems.
          precursors to the June 20 event, including the effectiveness of licensee actions
6.
          taken in response to the operating experience. As a minimum include Generic
Identify previous instrument air piping problems that may have been precursors
          Letter 88-14, Instrument Air Supply System Problems Affecting Safety-Related
to the June 20 event, including one event in 1994. Evaluate the licensees
          Equipment, including the licensees response to the generic letter; and NRC
corrective measures and extent of condition reviews for those problems.
          Information Notice 2002-29,Recent Design Problems in Safety Functions of
7.
          Pneumatic Systems. You may also use NUREG 1837, Regulatory
Evaluate the licensees instrument air system maintenance and testing
          Effectiveness Assessment of Generic Issue 43 and Generic Letter 88-14, to aid
programs. Verify that the programs are adequate and that the licensee is
          in your assessment. The NUREG can be found at:
following the program provisions. Pay particular attention to the historical health
          http://www.nrc.gov/reading-rm/doc-collections/nuregs/staff/sr1837/sr1837.pdf
of the instrument air compressors and piping system.
                                            A2-2                                Attachment 2
8.
Evaluate pertinent industry operating experience that represent potential
precursors to the June 20 event, including the effectiveness of licensee actions
taken in response to the operating experience. As a minimum include Generic
Letter 88-14, Instrument Air Supply System Problems Affecting Safety-Related
Equipment, including the licensees response to the generic letter; and NRC
Information Notice 2002-29,Recent Design Problems in Safety Functions of
Pneumatic Systems. You may also use NUREG 1837, Regulatory
Effectiveness Assessment of Generic Issue 43 and Generic Letter 88-14, to aid
in your assessment. The NUREG can be found at:
http://www.nrc.gov/reading-rm/doc-collections/nuregs/staff/sr1837/sr1837.pdf


  9.     Determine if there are any potential generic issues related to the failure of the
A2-3
          SONGS instrument air piping. Promptly communicate any potential generic
Attachment 2
          issues to Region IV management.
9.
  10.   Collect data as necessary to support a risk analysis. Work closely with the
Determine if there are any potential generic issues related to the failure of the
          Senior Reactor Analyst during this inspection.
SONGS instrument air piping. Promptly communicate any potential generic
C. Guidance
issues to Region IV management.
  Inspection Procedure 93812, Special Inspection, provides additional guidance to be
10.
  used by the Special Inspection Team. Your duties will be as described in Inspection
Collect data as necessary to support a risk analysis. Work closely with the
  Procedure 93812. The inspection should emphasize fact-finding in its review of the
Senior Reactor Analyst during this inspection.
  circumstances surrounding the event. It is not the responsibility of the team to examine
C.
  the regulatory process. Safety concerns identified that are not directly related to the
Guidance
  event should be reported to the Region IV office for appropriate action.
Inspection Procedure 93812, Special Inspection, provides additional guidance to be
  The Team will report to the site, conduct an entrance, and begin inspection no later than
used by the Special Inspection Team. Your duties will be as described in Inspection
  June 27, 2007. While on site, you will provide daily status briefings to Region IV
Procedure 93812. The inspection should emphasize fact-finding in its review of the
  management, who will coordinate with the Office of Nuclear Reactor Regulation, to
circumstances surrounding the event. It is not the responsibility of the team to examine
  ensure that all other parties are kept informed. A report documenting the results of the
the regulatory process. Safety concerns identified that are not directly related to the
  inspection should be issued within 30 days of the completion of the inspection.
event should be reported to the Region IV office for appropriate action.
  This Charter may be modified should the team develop significant new information that
The Team will report to the site, conduct an entrance, and begin inspection no later than  
  warrants review. Should you have any questions concerning this Charter, contact me at
June 27, 2007. While on site, you will provide daily status briefings to Region IV
  (817) 860-8147.
management, who will coordinate with the Office of Nuclear Reactor Regulation, to
                                          A2-3                                  Attachment 2
ensure that all other parties are kept informed. A report documenting the results of the
inspection should be issued within 30 days of the completion of the inspection.
This Charter may be modified should the team develop significant new information that
warrants review. Should you have any questions concerning this Charter, contact me at
(817) 860-8147.  


                                      ATTACHMENT 3
A3-1
                    SIGNIFICANCE DETERMINATION EVALUATION
Attachment 3
                          San Onofre Nuclear Generating Station
ATTACHMENT 3
                          Failure of Instrument Air System Header
SIGNIFICANCE DETERMINATION EVALUATION
                                      Phase 3 Analysis
San Onofre Nuclear Generating Station
A. Brief Description of Issue
Failure of Instrument Air System Header
  On June 20, 2007, instrument air pressure at San Onofre Unit 2 dropped significantly
Phase 3 Analysis
  following the separation of a 3-inch fitting in the system air header located in the
A.
  auxiliary building. This caused the feedwater control valves to stop functioning, resulting
Brief Description of Issue
  in an uncontrolled increase in steam generator water level. Operators manually tripped
On June 20, 2007, instrument air pressure at San Onofre Unit 2 dropped significantly
  the Unit 2 reactor. The loss of instrument air caused containment isolations and a loss
following the separation of a 3-inch fitting in the system air header located in the
  of most power conversion system functions.
auxiliary building. This caused the feedwater control valves to stop functioning, resulting
  The licensee performed a metallurgical analysis of the failed joint and determined that
in an uncontrolled increase in steam generator water level. Operators manually tripped
  the cause of the failure was poor workmanship during initial installation. The analysis
the Unit 2 reactor. The loss of instrument air caused containment isolations and a loss
  concluded that the joint was most likely leaking since initial plant startup because, during
of most power conversion system functions.
  original installation the brazing activity resulted in inadequate solder coverage and the
The licensee performed a metallurgical analysis of the failed joint and determined that
  connection had continued to deteriorate throughout the life of the plant. During a
the cause of the failure was poor workmanship during initial installation. The analysis
  walkdown of the system in both units, licensee personnel discovered that 32 other large
concluded that the joint was most likely leaking since initial plant startup because, during
  fittings were leaking at the joint.
original installation the brazing activity resulted in inadequate solder coverage and the
  A special inspection team reviewed the licensees root cause evaluation and
connection had continued to deteriorate throughout the life of the plant. During a
  metallurgical evaluation for this event. During their review, the team noted that there
walkdown of the system in both units, licensee personnel discovered that 32 other large
  had been a previous similar air header failure at San Onofre in June 1994. At that time,
fittings were leaking at the joint.
  both Units 2 and 3 experienced a loss of instrument air following the failure of an
  improperly soldered joint. A metallurgical analysis conducted in 1994 concluded that
A special inspection team reviewed the licensees root cause evaluation and
  this joint had also likely been leaking since initial startup from inadequate solder
metallurgical evaluation for this event. During their review, the team noted that there
  coverage.
had been a previous similar air header failure at San Onofre in June 1994. At that time,
  A large amount of industry operating experience has been available that deals with
both Units 2 and 3 experienced a loss of instrument air following the failure of an
  soldered joint issues. During the original evaluation of related operational experience
improperly soldered joint. A metallurgical analysis conducted in 1994 concluded that
  reports, done by the licensee in 1992, they failed to properly assess the impact to San
this joint had also likely been leaking since initial startup from inadequate solder
  Onofre. Engineers had determined that if failures were going to have occurred because
coverage.
  of inadequate fit-up and/or solder penetration, the failures would have occurred within a
A large amount of industry operating experience has been available that deals with
  relatively short time frame. Therefore, they assumed that related industry experience
soldered joint issues. During the original evaluation of related operational experience
  was not applicable to San Onofre. The team also determined that the licensee failed to
reports, done by the licensee in 1992, they failed to properly assess the impact to San
  adequately reassess their position when they experienced an air line joint failure in
Onofre. Engineers had determined that if failures were going to have occurred because
  1994, and as a result, failed to take effective corrective actions following that failure.
of inadequate fit-up and/or solder penetration, the failures would have occurred within a
B. Statement of the Performance Deficiency
relatively short time frame. Therefore, they assumed that related industry experience
  The licensee failed to take effective corrective actions in response to the failure of an
was not applicable to San Onofre. The team also determined that the licensee failed to
  improperly made soldered joint in the instrument air header affecting both units at San
adequately reassess their position when they experienced an air line joint failure in
                                            A3-1                                Attachment 3
1994, and as a result, failed to take effective corrective actions following that failure.
B.
Statement of the Performance Deficiency
The licensee failed to take effective corrective actions in response to the failure of an
improperly made soldered joint in the instrument air header affecting both units at San


  Onofre in June 1994. Specifically, contrary to Section 6.2.3 of
A3-2
  Procedure SO-123-I-1.42, Maintenance Division Experience Report, Revision 0, the
Attachment 3
  licensee failed to implement corrective actions to prevent recurrence for an equipment
Onofre in June 1994. Specifically, contrary to Section 6.2.3 of
  failure with the potential to cause a significant plant transient, and failed to appropriately
Procedure SO-123-I-1.42, Maintenance Division Experience Report, Revision 0, the
  consider previous industry and plant experience similar to the event. Additionally,
licensee failed to implement corrective actions to prevent recurrence for an equipment
  licensee personnel failed to properly evaluate and take corrective actions based on
failure with the potential to cause a significant plant transient, and failed to appropriately
  industry operating experience through 2006 involving improperly made soldered joints in
consider previous industry and plant experience similar to the event. Additionally,
  instrument air systems. As a result, an additional failure of an improperly made
licensee personnel failed to properly evaluate and take corrective actions based on
  instrument air header joint occurred at San Onofre on June 20, 2007, resulting in a
industry operating experience through 2006 involving improperly made soldered joints in
  complete loss of instrument air to Unit 2.
instrument air systems. As a result, an additional failure of an improperly made
C. Significance Determination Basis
instrument air header joint occurred at San Onofre on June 20, 2007, resulting in a
  1.     Phase 1 screening logic, results and assumptions
complete loss of instrument air to Unit 2.
          In accordance with NRC Inspection Manual Chapter 0612, Appendix B, "Issue
C.
          Screening," the team determined that this finding represented a licensee
Significance Determination Basis
          performance deficiency. The team then determined that the issue was more
1.
          than minor because the finding was associated with the equipment performance
Phase 1 screening logic, results and assumptions
          attribute and affected the initiating events cornerstone objective to limit the
In accordance with NRC Inspection Manual Chapter 0612, Appendix B, "Issue
          likelihood of those events that upset plant stability and challenge critical safety
Screening," the team determined that this finding represented a licensee
          functions during shutdown as well as power operations.
performance deficiency. The team then determined that the issue was more
          The team evaluated this finding using the, "SDP Phase 1 Screening Worksheet
than minor because the finding was associated with the equipment performance
          for the Initiating Events, Mitigating Systems, and Barriers Cornerstones,"
attribute and affected the initiating events cornerstone objective to limit the
          provided in Manual Chapter 0609, Appendix A, "Significance Determination of
likelihood of those events that upset plant stability and challenge critical safety
          Reactor Inspection Findings for At-Power Situations." A Phase 2 estimation was
functions during shutdown as well as power operations.
          required because the associated performance deficiency represented an
The team evaluated this finding using the, "SDP Phase 1 Screening Worksheet
          increase in both the likelihood of a reactor trip and the probability that the power
for the Initiating Events, Mitigating Systems, and Barriers Cornerstones,"
          conversion system would be unavailable.
provided in Manual Chapter 0609, Appendix A, "Significance Determination of
  2.     Phase 2 Risk Estimation
Reactor Inspection Findings for At-Power Situations." A Phase 2 estimation was
          In accordance with Manual Chapter 0609, Appendix A, Attachment 1, User
required because the associated performance deficiency represented an
          Guidance for Significance Determination of Reactor Inspection Findings for At-
increase in both the likelihood of a reactor trip and the probability that the power
          Power Situations, the team evaluated the subject findings using the Risk-
conversion system would be unavailable.
          Informed Inspection Notebook for San Onofre Nuclear Generating Station
2.
          (SONGS) Units 2 and 3, Revision 2.1. The dominant affected accident
Phase 2 Risk Estimation
          sequences are provided in Table 1. The team assumed that the exposure period
In accordance with Manual Chapter 0609, Appendix A, Attachment 1, User
          was greater than 30 days, that the performance deficiency increased the
Guidance for Significance Determination of Reactor Inspection Findings for At-
          likelihood that a complete loss of instrument air would occur, and that there was
Power Situations, the team evaluated the subject findings using the Risk-
          no affect on mitigating systems other than that modeled in the risk-informed
Informed Inspection Notebook for San Onofre Nuclear Generating Station
          notebook.
(SONGS) Units 2 and 3, Revision 2.1. The dominant affected accident
                                            A3-2                                    Attachment 3
sequences are provided in Table 1. The team assumed that the exposure period
was greater than 30 days, that the performance deficiency increased the
likelihood that a complete loss of instrument air would occur, and that there was
no affect on mitigating systems other than that modeled in the risk-informed
notebook.


                                          TABLE 1
A3-3
                Increased Likelihood of a Complete Loss of Instrument Air
Attachment 3
                                  Phase 2 Sequences
TABLE 1
      Initiating Event     Sequence             Mitigating Functions           Results
Increased Likelihood of a Complete Loss of Instrument Air
    Loss of Instrument     1             LOIA-AFW                             7
Phase 2 Sequences  
    Air
Initiating Event
                          2            LOIA-RCPTRIP-HPR                     9
Sequence
                          3             LOIA-RCPTRIP-CNT                     9
Mitigating Functions
                          4             LOIA-RCPTRIP-EIHP                     9
Results
  Using the counting rule worksheet, the result from this estimation indicated that
Loss of Instrument
  this finding was of very low safety significance (GREEN).
Air
  A senior reactor analyst reviewed the Phase 2 estimation and determined that
1
  the risk-informed notebook and the licensees PRA had a common error that
LOIA-AFW
  significantly underestimated the risk of this deficiency. The loss of instrument air
7
  initiating event frequency had been established as 6.4 x 10-5/year by assuming
2
  that a loss of all active instrument air system components as well as a loss of the
LOIA-RCPTRIP-HPR
  backup nitrogen system was required to realize a complete loss of instrument
9
  air. However, there are many system breaches and other passive component
3
  failures that would prevent the backup nitrogen system from performing its
LOIA-RCPTRIP-CNT
  function.
9
  Therefore, the analyst determined that the finding should be evaluated using the
4
  Phase 3 process.
LOIA-RCPTRIP-EIHP
3. Phase 3 Analysis
9
  The analyst quantified the change in risk of the subject performance deficiency
Using the counting rule worksheet, the result from this estimation indicated that
  as indicated in the paragraphs below. The change in internal event risk was
this finding was of very low safety significance (GREEN).
  estimated as 4.7 x 10-7 over an entire assessment period. The risk related to
A senior reactor analyst reviewed the Phase 2 estimation and determined that
  seismic events changed by 4.1 x 10-7 and that related to internal fires by
the risk-informed notebook and the licensees PRA had a common error that
  9.5 x 10-9. This resulted in a total change in CDF of 8.9 x 10-7. Therefore, the
significantly underestimated the risk of this deficiency. The loss of instrument air
  analyst determined that the subject finding was of very low safety significance
initiating event frequency had been established as 6.4 x 10-5/year by assuming
  (Green).
that a loss of all active instrument air system components as well as a loss of the
  Internal Initiating Events:
backup nitrogen system was required to realize a complete loss of instrument
  The following techniques were used in this evaluation.
air. However, there are many system breaches and other passive component
  a.       The analyst quantified the internal risk using the Standardized Plant
failures that would prevent the backup nitrogen system from performing its
            Analysis Risk (SPAR) Model for San Onofre 2 & 3, Revision 3.21, created
function.
            in October 2005. The analyst modeled a loss of instrument air by
Therefore, the analyst determined that the finding should be evaluated using the
            assuming that the affect was equivalent to a transient with a complete
Phase 3 process.
            loss of the power conversion system with the possibility of a recovery of
3.
                                    A3-3                                  Attachment 3
Phase 3 Analysis
The analyst quantified the change in risk of the subject performance deficiency
as indicated in the paragraphs below. The change in internal event risk was
estimated as 4.7 x 10-7 over an entire assessment period. The risk related to
seismic events changed by 4.1 x 10-7 and that related to internal fires by
9.5 x 10-9. This resulted in a total change in CDF of 8.9 x 10-7. Therefore, the
analyst determined that the subject finding was of very low safety significance
(Green).
Internal Initiating Events:
The following techniques were used in this evaluation.  
a.
The analyst quantified the internal risk using the Standardized Plant
Analysis Risk (SPAR) Model for San Onofre 2 & 3, Revision 3.21, created
in October 2005. The analyst modeled a loss of instrument air by
assuming that the affect was equivalent to a transient with a complete
loss of the power conversion system with the possibility of a recovery of


        condensate by bypassing the feedwater isolation and depressurizing the
A3-4
        steam generators. The likelihood of a loss of instrument air was then
Attachment 3
        increased to 6.8 x 10-2/year as a result of the performance deficiency.
condensate by bypassing the feedwater isolation and depressurizing the
        The resulting quantification indicated an increase over the baseline core
steam generators. The likelihood of a loss of instrument air was then
        damage frequency of 4.7 x 10-7 over a 365-day exposure.
increased to 6.8 x 10-2/year as a result of the performance deficiency.  
b.     The licensee developed a model for analyzing the internal risk associated
The resulting quantification indicated an increase over the baseline core
        with the event using the current version of their PRA model. The licensee
damage frequency of 4.7 x 10-7 over a 365-day exposure.
        revised the model by setting the loss of instrument air initiating event
b.
        frequency to 0.5 indicating that operators could have recovered the
The licensee developed a model for analyzing the internal risk associated
        condition prior to a reactor trip. Additionally, the licensee estimated that
with the event using the current version of their PRA model. The licensee
        50% of the transients initiated by an instrument air system breach would
revised the model by setting the loss of instrument air initiating event
        be recovered by operators prior to core damage. No other initiators were
frequency to 0.5 indicating that operators could have recovered the
        considered to be applicable to this condition.
condition prior to a reactor trip. Additionally, the licensee estimated that
        Licensee analysts changed their model to show that the controlled
50% of the transients initiated by an instrument air system breach would
        bleedoff valves remained open. As documented in Licensee Event
be recovered by operators prior to core damage. No other initiators were
        Report 50-361/2007001, the licensees conditional core damage
considered to be applicable to this condition.
        probability (CCDP) for this event was 3.3 x 10-6.
Licensee analysts changed their model to show that the controlled
        At the analysts request, the licensee provided a CCDP for a generic loss
bleedoff valves remained open. As documented in Licensee Event
        of instrument air. The value provided by their model was 4.85 x 10-6.
Report 50-361/2007001, the licensees conditional core damage
        The analyst converted the licensees CCDP to a change in the core
probability (CCDP) for this event was 3.3 x 10-6.
        damage frequency by multiplying it with the calculated initiating event
At the analysts request, the licensee provided a CCDP for a generic loss
        frequency. The result was 3.29 x 10-7 over the 1-year assessment
of instrument air. The value provided by their model was 4.85 x 10-6.  
        period. This tends to corroborate the analysts value and suggests that
The analyst converted the licensees CCDP to a change in the core
        the initiating event frequency is the primary difference between the two
damage frequency by multiplying it with the calculated initiating event
        values.
frequency. The result was 3.29 x 10-7 over the 1-year assessment
period. This tends to corroborate the analysts value and suggests that
the initiating event frequency is the primary difference between the two
values.
In performing the Phase 3 evaluation, the following influential assumptions were
In performing the Phase 3 evaluation, the following influential assumptions were
made by the analyst:
made by the analyst:
a.     The failure of a large fitting in the instrument air system at the San
a.
        Onofre site would cause a reactor trip on the subject unit at least 1/2 the
The failure of a large fitting in the instrument air system at the San
        time. This was based on the 2 historical failures in the units.
Onofre site would cause a reactor trip on the subject unit at least 1/2 the
b.     This condition existed for many years for both units and should be
time. This was based on the 2 historical failures in the units.
        evaluated over the most recent 1-year assessment period.
b.
c.     The baseline failure rate of the instrument air system should have been
This condition existed for many years for both units and should be
        the boolean combination of the system components including the backup
evaluated over the most recent 1-year assessment period.
        instrument air system. Given intact system piping, this was calculated by
c.
        the licensee to be 6.4 x 10-5/year.
The baseline failure rate of the instrument air system should have been
d.     The instrument air system had been functional for 22.09 reactor-years.
the boolean combination of the system components including the backup
        This value is the number of years that either or both reactors were critical.
instrument air system. Given intact system piping, this was calculated by
        Such an assumption was used because the system is common to both
the licensee to be 6.4 x 10-5/year.
        units.
d.
                                  A3-4                                  Attachment 3
The instrument air system had been functional for 22.09 reactor-years.  
This value is the number of years that either or both reactors were critical.  
Such an assumption was used because the system is common to both
units.


e.     Because the condition causing failures in the instrument air headers was,
A3-5
        in part, an aging issue and because there were 32 additional leaking
Attachment 3
        fittings identified in the system, the analyst assumed that an additional
e.
        failure was eminent prior to repair (eg: 3 failures were assumed to have
Because the condition causing failures in the instrument air headers was,
        occurred).
in part, an aging issue and because there were 32 additional leaking
f.     Upon loss of instrument air, the condensate system is potentially still
fittings identified in the system, the analyst assumed that an additional
        available given operators depressurize the reactor coolant system and
failure was eminent prior to repair (eg: 3 failures were assumed to have
        manually realign the condensate system to bypass the feedwater
occurred).
        regulating valves.
f.
Upon loss of instrument air, the condensate system is potentially still
available given operators depressurize the reactor coolant system and
manually realign the condensate system to bypass the feedwater
regulating valves.
The following calculations were performed during this analysis:
The following calculations were performed during this analysis:
a.     The analyst calculated the revised likelihood of a loss of instrument air.
a.
        The result of 1.36 x 10-1 was calculated based on the 2 historical
The analyst calculated the revised likelihood of a loss of instrument air.  
        breaches of the system, an additional postulated breach to account for
The result of 1.36 x 10-1 was calculated based on the 2 historical
        the aging affect, and a service time of 22.09 reactor-years.
breaches of the system, an additional postulated breach to account for
b.     As stated above, historically San Onofre has had 2 events that involved
the aging affect, and a service time of 22.09 reactor-years.
        breaches of an instrument air header. On one of these occasions,
b.
        operators were able to identify and limit the leak to prevent a reactor
As stated above, historically San Onofre has had 2 events that involved
        transient. Therefore, the initiating event likelihood was reduced by 50%
breaches of an instrument air header. On one of these occasions,
        to 6.8 x 10-2.
operators were able to identify and limit the leak to prevent a reactor
c.     The analyst estimated the nonrecovery probability for the operators
transient. Therefore, the initiating event likelihood was reduced by 50%
        depressurizing the reactor coolant system and feeding the steam
to 6.8 x 10-2.
        generators using the condensate system. Three components went into
c.
        this analysis: 1) the human error probability calculated using the SPAR-H
The analyst estimated the nonrecovery probability for the operators
        method; 2) the probability that the atmospheric dump system failed; and
depressurizing the reactor coolant system and feeding the steam
        3) the probability that the condensate system failed mechanically. The
generators using the condensate system. Three components went into
        last two probabilities were calculated by solving appropriate portions of
this analysis: 1) the human error probability calculated using the SPAR-H
        the SPAR fault trees. The overall nonrecovery probability was calculated
method; 2) the probability that the atmospheric dump system failed; and
        to be 9.3 x 10-2.
3) the probability that the condensate system failed mechanically. The
d.     The analyst used the SPAR model to quantify the internal change in risk
last two probabilities were calculated by solving appropriate portions of
        for a loss of instrument air by modeling a loss of condensate, bypass
the SPAR fault trees. The overall nonrecovery probability was calculated
        capability, and main feedwater. The analyst set all initiators to the house
to be 9.3 x 10-2.
        event, FALSE, with the exception of transients. The transient initiator
d.
        was used as a surrogate initiator for the loss of instrument air, and the
The analyst used the SPAR model to quantify the internal change in risk
        initiating event frequency was set to the calculated frequency above.
for a loss of instrument air by modeling a loss of condensate, bypass
        The analyst also provided for recovery of the condensate system by
capability, and main feedwater. The analyst set all initiators to the house
        adding a basic event to the COND fault tree. This basic event COND-
event, FALSE, with the exception of transients. The transient initiator
        RECOVERY was added under the AND gate, COND-SYS-4. This gate
was used as a surrogate initiator for the loss of instrument air, and the
        then indicated that the failure of both feedwater pathways as well as
initiating event frequency was set to the calculated frequency above.
        nonrecovery of the condensate system via the alternate pathway were
The analyst also provided for recovery of the condensate system by
        required to fail the condensate function.
adding a basic event to the COND fault tree. This basic event COND-
                                  A3-5                                Attachment 3
RECOVERY was added under the AND gate, COND-SYS-4. This gate
then indicated that the failure of both feedwater pathways as well as
nonrecovery of the condensate system via the alternate pathway were
required to fail the condensate function.


A3-6
Attachment 3
The changes to basic events used for this model are shown on Table 2.
The changes to basic events used for this model are shown on Table 2.
                                TABLE 2
TABLE 2
              Changes to SPAR Model Basic Events
Changes to SPAR Model Basic Events  
          Basic Event             Initial Value   Adjusted Value
Basic Event
    IE-TRANS                     7.0 x 10-1       6.8 x 10-2
Initial Value
    All Other Initiators         Nominal           FALSE
Adjusted Value
    MFW-AOV-CF-SGS               2.7 x 10-5       TRUE
IE-TRANS
    MFW-AOV-OC-4048             7.2 x 10-6       TRUE
7.0 x 10-1
    MFW-AOV-OC-4052             7.2 x 10-6       TRUE
6.8 x 10-2
    MFW-SYS-AVAILABLE           0.8               1.0
All Other Initiators
    MFW-SYS-UNAVAIL             0.2               FALSE
Nominal
    MSS-TBV-CF-TBVS             2.6 x 10-6       TRUE
FALSE
    COND-RECOVERY               N/A               9.3 x 10-2
MFW-AOV-CF-SGS
The model was then quantified. The case core damage frequency (CDF)
2.7 x 10-5
TRUE
MFW-AOV-OC-4048
7.2 x 10-6
TRUE
MFW-AOV-OC-4052
7.2 x 10-6
TRUE
MFW-SYS-AVAILABLE
0.8
1.0
MFW-SYS-UNAVAIL
0.2
FALSE
MSS-TBV-CF-TBVS
2.6 x 10-6
TRUE
COND-RECOVERY
N/A
9.3 x 10-2
The model was then quantified. The case core damage frequency (CDF)
was computed to be 4.7 x 10-7/year and the baseline CDF, using the
was computed to be 4.7 x 10-7/year and the baseline CDF, using the
baseline initiating event frequency of 6.4 x 10-5/year, was computed to be
baseline initiating event frequency of 6.4 x 10-5/year, was computed to be
4.1 x 10-10/year. The change in CDF (CDF) was then calculated by
4.1 x 10-10/year. The change in CDF (CDF) was then calculated by
subtracting the baseline CDF from the case CDF. This resulted in a
subtracting the baseline CDF from the case CDF. This resulted in a
CDF for the increased likelihood for a loss of instrument air of 4.7 x 10-7
CDF for the increased likelihood for a loss of instrument air of 4.7 x 10-7
over a 365-day exposure. The dominant sequences from the SPAR and
over a 365-day exposure. The dominant sequences from the SPAR and
licensee models are documented in Table 3.
licensee models are documented in Table 3.
                                    Table 3
Table 3
                    Phase 3 Dominant Accident Sequences
Phase 3 Dominant Accident Sequences
  Model           Initiating Event         Sequence         Contribution
Model
  SPAR 3.21       Loss of Instrument Air   AFW,               4.5 x 10-7
Initiating Event
                                            Condensate
Sequence
  Licensee's     Loss of Instrument Air   AFW, Failure to     3.1 x 10-7
Contribution
  Revised                                  Depressurize
SPAR 3.21
                          A3-6                                Attachment 3
Loss of Instrument Air
AFW,
Condensate
4.5 x 10-7
Licensee's
Revised
Loss of Instrument Air
AFW, Failure to
Depressurize
3.1 x 10-7


A3-7
Attachment 3
External Initiating Events:
External Initiating Events:
The analyst used the following methods for determining the change in risk from
The analyst used the following methods for determining the change in risk from
external events. The change in risk from an increase in the frequency of a loss
external events. The change in risk from an increase in the frequency of a loss
of instrument air was estimated to be 4.2 x 10-7 for a 365-day period. The
of instrument air was estimated to be 4.2 x 10-7 for a 365-day period. The
methods used are documented below:
methods used are documented below:
a.     Fire
a.
        The analyst used the San Onofre IPEEE to estimate the change in risk
Fire
        resulting from internal fire. The only fire areas where risk could be
The analyst used the San Onofre IPEEE to estimate the change in risk
        increased by the subject improperly soldered fittings would be those
resulting from internal fire. The only fire areas where risk could be
        containing instrument air header piping. As the limiting area, the analyst
increased by the subject improperly soldered fittings would be those
        reviewed the licensees evaluation of Fire Area 2-TB-148. The fire
containing instrument air header piping. As the limiting area, the analyst
        ignition frequency for this area was 4.5 x 10-2/yr. The analyst assumed
reviewed the licensees evaluation of Fire Area 2-TB-148. The fire
        that only 0.1 of the fires would grow to a size that could impact the
ignition frequency for this area was 4.5 x 10-2/yr. The analyst assumed
        instrument air system (severity factor) and that about 50 percent of the
that only 0.1 of the fires would grow to a size that could impact the
        fires would cause a weakening of the improperly soldered fitting joints
instrument air system (severity factor) and that about 50 percent of the
        without causing baseline failure of the system. Using a conditional core
fires would cause a weakening of the improperly soldered fitting joints
        damage probability of 4.2 x 10-6, the change in core damage frequency
without causing baseline failure of the system. Using a conditional core
        from the subject performance deficiency related to a turbine building fire
damage probability of 4.2 x 10-6, the change in core damage frequency
        was estimated as 9.5 x 10-9 over the 365-day exposure period.
from the subject performance deficiency related to a turbine building fire
b.     Seismic
was estimated as 9.5 x 10-9 over the 365-day exposure period.
        The analyst determined that, for the subject performance deficiency to
b.
        affect the core damage frequency, a seismic event must result in a failure
Seismic
        of an instrument air system header fitting without otherwise affecting
The analyst determined that, for the subject performance deficiency to
        instrument air system components.
affect the core damage frequency, a seismic event must result in a failure
        To estimate the baseline seismic failure of the system, the analyst used
of an instrument air system header fitting without otherwise affecting
        the seismic fragility of the air-operated valves which were the least
instrument air system components.
        durable components in the system as designed. The analyst evaluated
 
        the subject performance deficiency by determining each of the following
To estimate the baseline seismic failure of the system, the analyst used
        parameters for any seismic event producing a given range of median
the seismic fragility of the air-operated valves which were the least
        acceleration "a" [SE(a)]:
durable components in the system as designed. The analyst evaluated
                1.     The frequency of the seismic event SE(a) (SE(a)) ;
the subject performance deficiency by determining each of the following
                2.     The probability that a system header fitting fails (PHeader-SE(a));
parameters for any seismic event producing a given range of median
                3.     The probability that an air-operated valve fails (P System-SE(a));
acceleration "a" [SE(a)]:
                4.     The conditional change in CDP (CCDPSE(a))
1.
        The CDF for the acceleration range in question (CDFSE(a)) can then be
The frequency of the seismic event SE(a) (SE(a)) ;
        quantified as follows:
2.
                CDFSE(a) = SE(a) * PHeader-SE(a) * (1 - PSystem-SE(a)) * CCDPSE(a)
The probability that a system header fitting fails (PHeader-SE(a));
                                    A3-7                                    Attachment 3
3.
The probability that an air-operated valve fails (P System-SE(a));
4.
The conditional change in CDP (CCDPSE(a))
The CDF for the acceleration range in question (CDFSE(a)) can then be
quantified as follows:
CDFSE(a) = SE(a) * PHeader-SE(a) * (1 - PSystem-SE(a)) * CCDPSE(a)


A3-8
Attachment 3
Given that each range a was selected by the analyst specifically to be
Given that each range a was selected by the analyst specifically to be
independent of all other ranges, the total increase in risk, CDF, can be
independent of all other ranges, the total increase in risk, CDF, can be
quantified by summing the CDFSE(a) for each range evaluated as follows:
quantified by summing the CDFSE(a) for each range evaluated as follows:
                  6
  6
        CDF = 3 CDFSE(a)
CDF = 3   CDFSE(a)
                  a=.03
  a=.03
over the range of SE(a).
over the range of SE(a).
1.     Frequency of the Seismic Event
1.
        NRC research data indicated that seismic events of 0.05g or less have
Frequency of the Seismic Event
        little to no impact on internal plant equipment. The analyst assumed
NRC research data indicated that seismic events of 0.05g or less have
        that seismic events less than 0.03g do not directly affect the plant.
little to no impact on internal plant equipment. The analyst assumed
        The analyst assumed that seismic events greater than 6.0g lead to
that seismic events less than 0.03g do not directly affect the plant.  
        core damage. The analyst therefore examined seismic events in the
The analyst assumed that seismic events greater than 6.0g lead to
        range of 0.03g to 6.0g.
core damage. The analyst therefore examined seismic events in the
        The analyst divided that range of seismic events into segments (called
range of 0.03g to 6.0g.
        "bins" hereafter); specifically, seismic events from 0.03g to 0.1g were
The analyst divided that range of seismic events into segments (called
        binned by hundredths, seismic events from 0.1g to 1.0g were binned
"bins" hereafter); specifically, seismic events from 0.03g to 0.1g were
        by tenths, and seismic events from 1.0g to 6.0g were binned by ones.
binned by hundredths, seismic events from 0.1g to 1.0g were binned
        In order to determine the frequency of a seismic event for a specific
by tenths, and seismic events from 1.0g to 6.0g were binned by ones.
        range of ground motion (g values), the analyst used a plot provided by
In order to determine the frequency of a seismic event for a specific
        the licensee and obtained values for the frequency of the seismic
range of ground motion (g values), the analyst used a plot provided by
        event that generates a level of ground motion (in peak ground
the licensee and obtained values for the frequency of the seismic
        acceleration) that exceeds the lower value in each of the bins. The
event that generates a level of ground motion (in peak ground
        analyst then calculated the difference in these frequency of
acceleration) that exceeds the lower value in each of the bins. The
        exceedance values to obtain the frequency of seismic events for the
analyst then calculated the difference in these frequency of
        binned seismic event ranges.
exceedance values to obtain the frequency of seismic events for the
        For example, according to the San Onofre curves, the frequency of
binned seismic event ranges.
        exceedance for a 0.6g seismic event is estimated at 3.9 x 10-2/yr and a
For example, according to the San Onofre curves, the frequency of
        0.7g seismic event at 3.5 x 10-2/yr. The frequency of seismic events
exceedance for a 0.6g seismic event is estimated at 3.9 x 10-2/yr and a
        with median acceleration in the range of 0.6g to 0.7g [SE(0.6-0.7)]
0.7g seismic event at 3.5 x 10-2/yr. The frequency of seismic events
        equals the difference, or 4.0 x 10-3/yr.
with median acceleration in the range of 0.6g to 0.7g [SE(0.6-0.7)]
2.     Probability of a Header Fitting Failure
equals the difference, or 4.0 x 10-3/yr.
        Given that the historical header failures were the result of insufficient
2.
        solder coverage and were caused by slow degradation via air leaks,
Probability of a Header Fitting Failure
        the analyst assumed that a moderately large earthquake could result
Given that the historical header failures were the result of insufficient
        in the failure of a leaking header fitting. Therefore, the analyst used a
solder coverage and were caused by slow degradation via air leaks,
        median seismic fragility of a long, brittle component as an estimate of
the analyst assumed that a moderately large earthquake could result
        the fragility of the 32 degraded instrument air header fittings. The
in the failure of a leaking header fitting. Therefore, the analyst used a
        seismic fragility selected was 0.3g.
median seismic fragility of a long, brittle component as an estimate of
                            A3-8                                Attachment 3
the fragility of the 32 degraded instrument air header fittings. The
seismic fragility selected was 0.3g.


A3-9
Attachment 3
The analyst obtained data on switchyard components from the Risk
The analyst obtained data on switchyard components from the Risk
Assessment of Operating Events Handbook; Volume 2, External
Assessment of Operating Events Handbook; Volume 2, External
Events, Revision 4, which referenced generic fragility values listed in:
Events, Revision 4, which referenced generic fragility values listed in:
<         NUREG/CR-6544, Methodology for Analyzing Precursors to
<
          Earthquake-Initiated and Fire-Initiated Accident Sequences,
NUREG/CR-6544, Methodology for Analyzing Precursors to
          April 1998; and
Earthquake-Initiated and Fire-Initiated Accident Sequences,
<         NUREG/CR-4550, Vols 3 and 4 part 3, Analysis of Core
April 1998; and
          Damage Frequency: Surry / Peach Bottom, 1986
<
NUREG/CR-4550, Vols 3 and 4 part 3, Analysis of Core
Damage Frequency: Surry / Peach Bottom, 1986
The references describe the mean failure probability for various
The references describe the mean failure probability for various
equipment using the following equation:
equipment using the following equation:
          Pfail(a) =  [ ln(a/am) / (r2 + u2)1/2]
Pfail(a) =  [ ln(a/am) / (r
          Where  is the standard normal cumulative distribution
2 + u
          function and
2)1/2]
          a=       median acceleration level of the seismic event;
Where  is the standard normal cumulative distribution
          am=     median of the component fragility;
function and
          r=     logarithmic standard deviation representing random
a =  
                  uncertainty;
median acceleration level of the seismic event;
          u =     logarithmic standard deviation representing systematic
am=
                  or modeling uncertainty.
median of the component fragility;  
r=
logarithmic standard deviation representing random
uncertainty;
u=
logarithmic standard deviation representing systematic
or modeling uncertainty.
In order to calculate the probability that a degraded fitting would fail
In order to calculate the probability that a degraded fitting would fail
given a seismic event, the analyst used the following generic seismic
given a seismic event, the analyst used the following generic seismic
fragilities:
fragilities:
          am = 0.3g
am = 0.3g
          r = 0.30
r = 0.30
          u = 0.45
u = 0.45
Using the above normal cumulative distribution function equation the
Using the above normal cumulative distribution function equation the
analyst determined the conditional probability of failure given a seismic
analyst determined the conditional probability of failure given a seismic
event. For each of the bins the calculation was performed substituting
event. For each of the bins the calculation was performed substituting
for the variable "a" (median acceleration level) the acceleration levels
for the variable "a" (median acceleration level) the acceleration levels
obtained from the bins described above. The following table shows
obtained from the bins described above. The following table shows
the results of the calculation for various acceleration levels.
the results of the calculation for various acceleration levels.
              Median Acceleration Level/Probability of Failure
Median Acceleration Level/Probability of Failure
    0.03g     3.6 x 10-5     0.3g   6.1 x 10-1   1.0g   1.0
0.03g
    0.07g     5.2 x 10-3     0.7g   9.5 x 10-1
3.6 x 10-5
                      A3-9                                Attachment 3
0.3g
6.1 x 10-1
1.0g
1.0
0.07g
5.2 x 10-3
0.7g
9.5 x 10-1


3. Probability that Air-Operated Valves Fail
A3-10
  In order to calculate the probability that the instrument air system
Attachment 3
  would fail during a given seismic event for reasons other than
3.
  improperly soldered fittings, the analyst used the following generic
Probability that Air-Operated Valves Fail
  seismic fragilities for air-operated valves:
In order to calculate the probability that the instrument air system
            am = 3.8g
would fail during a given seismic event for reasons other than
            r = 0.35
improperly soldered fittings, the analyst used the following generic
            u = 0.50
seismic fragilities for air-operated valves:
  Using the above standard normal cumulative distribution function
am = 3.8g
  equation, the analyst determined the conditional probability that the
r = 0.35
  instrument air system would fail from failure of system valves given a
u = 0.50
  seismic event for each of the bins. The calculation was performed
Using the above standard normal cumulative distribution function
  substituting for the variable "a" (median acceleration level) the
equation, the analyst determined the conditional probability that the
  acceleration levels obtained from the bins described above. The
instrument air system would fail from failure of system valves given a
  following table shows the results of the calculation for various
seismic event for each of the bins. The calculation was performed
  acceleration levels.
substituting for the variable "a" (median acceleration level) the
                          Median Acceleration Level/
acceleration levels obtained from the bins described above. The
                  Probability of Air-Operated Valve Failure
following table shows the results of the calculation for various
      0.03g   7.9 x 10-15     0.3g   4.7 x 10-5     1.0g     6.4 x 10-2
acceleration levels.
      0.07g   6.3 x 10-11     0.7g   3.9 x 10-3
Median Acceleration Level/
4. Conditional Change in Core Damage Probability
Probability of Air-Operated Valve Failure
  The analyst evaluated the spectrum of seismic initiators to determine
0.03g
  the resultant impact on the reliability and availability of mitigating
7.9 x 10-15
  systems affecting the subject performance deficiency.
0.3g
  The analyst used the SPAR model, to perform the Phase 3 evaluation.
4.7 x 10-5
  The analyst started with the model discussed above used to quantify
1.0g
  the change in risk from internal events. However, the analyst set the
6.4 x 10-2
  initiating event frequency for a transient to 1.0 and all other initiating
0.07g
  event probabilities in the SPAR model to zero. Because of the very
6.3 x 10-11
  narrow time windows discussed for condensate recovery, and the
0.7g
  added burdens on operators both emotionally and physically following
3.9 x 10-3
  a seismic event, the analyst set the nonrecovery probability for the
4.
  condensate system to 1.0. The SPAR model showed the resultant
Conditional Change in Core Damage Probability
  core damage probability as 1.02 x 10-4, which represented the value
The analyst evaluated the spectrum of seismic initiators to determine
  used in the above equation.
the resultant impact on the reliability and availability of mitigating
                      A3-10                                Attachment 3
systems affecting the subject performance deficiency.
The analyst used the SPAR model, to perform the Phase 3 evaluation.  
The analyst started with the model discussed above used to quantify
the change in risk from internal events. However, the analyst set the
initiating event frequency for a transient to 1.0 and all other initiating
event probabilities in the SPAR model to zero. Because of the very
narrow time windows discussed for condensate recovery, and the
added burdens on operators both emotionally and physically following
a seismic event, the analyst set the nonrecovery probability for the
condensate system to 1.0. The SPAR model showed the resultant
core damage probability as 1.02 x 10-4, which represented the value
used in the above equation.


                The SPAR Model was then requantified indicating no loss of
A3-11
                instrument air. The CCDP for this baseline condition was 4.35 x 10-7.
Attachment 3
                Therefore, the change in core damage probability is:
The SPAR Model was then requantified indicating no loss of
                          CCDPSE(a) = 1.02 x 10-4 - 4.35 x 10-7 = 1.02 x 10-4
instrument air. The CCDP for this baseline condition was 4.35 x 10-7.  
        Phase 3 Seismic Results
Therefore, the change in core damage probability is:
        Given the assumptions previously discussed, the total increase in core
CCDPSE(a) = 1.02 x 10-4 - 4.35 x 10-7 = 1.02 x 10-4
        damage frequency was estimated to be about 4.1 x 10-7 for seismic events
Phase 3 Seismic Results
        ranging from 0.03g to 6.0g.
Given the assumptions previously discussed, the total increase in core
c.     Winds, Floods, and Other External Events
damage frequency was estimated to be about 4.1 x 10-7 for seismic events
        The analyst reviewed the IPEEE and determined that no other credible
ranging from 0.03g to 6.0g.
        scenarios initiated by high winds, floods, fire, and other external events could
 
        initiate a failure of the degraded instrument air header fittings. Therefore, the
c.
        analyst concluded that external events other than internal fires and seismic
Winds, Floods, and Other External Events
        events were not significant contributors to risk for this finding.
The analyst reviewed the IPEEE and determined that no other credible
scenarios initiated by high winds, floods, fire, and other external events could
initiate a failure of the degraded instrument air header fittings. Therefore, the
analyst concluded that external events other than internal fires and seismic
events were not significant contributors to risk for this finding.
Risk Contribution from Large Early Release Frequency (LERF):
Risk Contribution from Large Early Release Frequency (LERF):
Using IMC 0609 Appendix H, the SRA determined that this was a Type A finding for a
Using IMC 0609 Appendix H, the SRA determined that this was a Type A finding for a
large dry containment. For PWR plants with large dry containments, only findings
large dry containment. For PWR plants with large dry containments, only findings
related to accident categories ISLOCA and SGTR have the potential to impact LERF.
related to accident categories ISLOCA and SGTR have the potential to impact LERF.  
In addition, an important insight from the IPE program and other PRAs is that the
In addition, an important insight from the IPE program and other PRAs is that the
conditional probability of early containment failure is less than 0.1 for core damage
conditional probability of early containment failure is less than 0.1 for core damage
scenarios that leave the RCS at high pressure (>250 psi) at the time of reactor vessel
scenarios that leave the RCS at high pressure (>250 psi) at the time of reactor vessel
breach. Since this finding is not related to ISLOCA or SGTR, and the core damage
breach. Since this finding is not related to ISLOCA or SGTR, and the core damage
scenarios for this finding leave the RCS at high pressure, the analyst concluded that
scenarios for this finding leave the RCS at high pressure, the analyst concluded that
LERF is not a significant contributor to the risk associated with this finding.
LERF is not a significant contributor to the risk associated with this finding.
                                    A3-11                                Attachment 3
}}
}}

Latest revision as of 21:29, 14 January 2025

IR 05000361-07-013, 05000362-07-013, on 06/27/07 - 07/02/07, San Onofre Nuclear Generating Station, Units 2, 3, and Independent Spent Fuel Storage Installation; Special Inspection in Response to an Instrument Air Header Break and Unit 2 Tri
ML072950104
Person / Time
Site: San Onofre  Southern California Edison icon.png
Issue date: 10/19/2007
From: Clark J
NRC/RGN-IV/DRP/RPB-E
To: Rosenblum R
Southern California Edison Co
References
IR-07-013
Download: ML072950104 (76)


See also: IR 05000361/2007013

Text

October 19, 2007

Richard M. Rosenblum

Senior Vice President and

Chief Nuclear Officer

Southern California Edison Company

San Onofre Nuclear Generating Station

P.O. Box 128

San Clemente, CA 92674-0128

SUBJECT:

SAN ONOFRE NUCLEAR GENERATING STATION - NRC SPECIAL

INSPECTION REPORT 05000361/2007013; 05000362/2007013

Dear Mr. Rosenblum:

On September 13, 2007, the U.S. Nuclear Regulatory Commission (NRC) completed a special

inspection at your San Onofre Nuclear Generating Station facility. This inspection examined

activities associated with the loss of instrument air event on June 20, 2007. On this occasion,

instrument air pressure on Unit 2 dropped significantly, causing the feedwater control valves to

stop functioning and resulting in an increase in steam generator water level. Operators

manually tripped the Unit 2 reactor. The NRC's initial evaluation satisfied the criteria in NRC

Management Directive 8.3, NRC Incident Investigation Program, for conducting a special

inspection. The basis for initiating this special inspection is further discussed in the inspection

charter, which is included in this report as Attachment 2. The determination that the inspection

would be conducted was made by the NRC on June 26, 2007, and the inspection started on

June 27, 2007.

The enclosed inspection report documents the inspection findings, which were discussed on

September 13, 2007 and again on October 11, 2007, with members of your staff. The

inspection examined activities conducted under your license as they relate to safety and

compliance with the Commission's rules and regulations and with the conditions of your license.

The inspectors reviewed selected procedures and records, observed activities, and interviewed

personnel.

The report documents eight NRC identified and self-revealing findings of very low safety

significance (Green). The eight findings involved issues concerning both the failure of your

processes and programs to prevent or mitigate the loss of instrument air event, and the

subsequent failure of your staff to thoroughly evaluate operator and equipment responses

following the event. The NRC is concerned about the occurrence of this event and the less

than adequate reviews conducted by your staff, and will conduct followup baseline inspections

to verify that your corrective actions in response to this inspection are thorough and effective.

Five of the findings were determined to involve violations of NRC requirements. Because of

their very low safety significance and because they were entered into your corrective action

program, the NRC is treating these findings as noncited violations (NCVs) consistent with

Section VI.A.1 of the NRC Enforcement Policy. If you contest these NCVs, you should provide

Southern California Edison Company

- 2 -

a response within 30 days of the date of this inspection report, with the basis for your denial, to

the U.S. Nuclear Regulatory Commission, ATTN: Document Control Desk, Washington

DC 20555-0001; with copies to the Regional Administrator, U.S. Nuclear Regulatory

Commission Region IV, 611 Ryan Plaza Drive, Suite 400, Arlington, Texas, 76011-4005; the

Director, Office of Enforcement, U.S. Nuclear Regulatory Commission, Washington

DC 20555-0001; and the NRC Resident Inspector at the San Onofre Nuclear Generating

Station facility.

In accordance with 10 CFR 2.390 of the NRC's Rules of Practice, a copy of this letter, its

enclosure, and your response (if any) will be made available electronically for public inspection

in the NRC Public Document Room or from the Publicly Available Records (PARS) component

of NRCs document system (ADAMS). ADAMS is accessible from the NRC Web site at

http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room).

Sincerely,

/RA/

Jeffrey A. Clark, Chief

Projects Branch E

Division of Reactor Projects

Dockets: 50-361

50-362

License: NPF-10

NPF-15

Enclosure: Inspection Report 05000361/2007013; 05000362/2007013

Attachment 1: Supplemental Information

Attachment 2: Special Inspection Charter

Attachment 3: Significance Determination Evaluation

cc w/Enclosure:

Chairman, Board of Supervisors

County of San Diego

1600 Pacific Highway, Room 335

San Diego, CA 92101

Gary L. Nolff

Assistant Director-Resources

City of Riverside

3900 Main Street

Riverside, CA 92522

Mark L. Parsons

Deputy City Attorney

City of Riverside

3900 Main Street

Riverside, CA 92522

Dr. David Spath, Chief

Division of Drinking Water and

Environmental Management

California Department of Health Services

850 Marina Parkway, Bldg P, 2nd Floor

Richmond, CA 94804

Michael J. DeMarco

San Onofre Liaison

San Diego Gas & Electric Company

8315 Century Park Ct. CP21G

San Diego, CA 92123-1548

Director, Radiological Health Branch

State Department of Health Services

P.O. Box 997414 (MS 7610)

Sacramento, CA 95899-7414

Southern California Edison Company

- 3 -

Mayor

City of San Clemente

100 Avenida Presidio

San Clemente, CA 92672

James D. Boyd, Commissioner

California Energy Commission

1516 Ninth Street (MS 34)

Sacramento, CA 95814

Douglas K. Porter, Esq.

Southern California Edison Company

2244 Walnut Grove Avenue

Rosemead, CA 91770

Mr. Raymond W. Waldo, Vice President,

Nuclear Generation

Southern California Edison Company

San Onofre Nuclear Generating Station

P.O. Box 128

San Clemente, CA 92674-0128

A. Edward Scherer

Southern California Edison Company

San Onofre Nuclear Generating Station

P.O. Box 128

San Clemente, CA 92674-0128

Brian Katz

Southern California Edison Company

San Onofre Nuclear Generating Station

P.O. Box 128

San Clemente, CA 92674-0128

Mr. Steve Hsu

Department of Health Services

Radiologic Health Branch

MS 7610, P.O. Box 997414

Sacramento, CA 95899-7414

Mr. James T. Reilly

Southern California Edison Company

San Onofre Nuclear Generating Station

P.O. Box 128

San Clemente, CA 92674-0128

Southern California Edison Company

- 4 -

Electronic distribution by RIV:

Regional Administrator (EEC)

DRP Director (ATH)

DRS Director (DDC)

DRS Deputy Director (RJC1)

Senior Resident Inspector (CCO1)

Branch Chief, DRP/E (JAC)

Senior Project Engineer, DRP/E (GDR)

Team Leader, DRP/TSS (CJP)

RITS Coordinator (MSH3)

Only inspection reports to the following:

DRS STA (DAP)

V. Dricks, PAO (VLD)

D. Pelton, OEDO RIV Coordinator (DLP)

ROPreports

SO Site Secretary (vacant)

SUNSI Review Completed: _JAC__ ADAMS:  : Yes

G No Initials: __JAC_

Publicly Available G Non-Publicly Available G Sensitive
Non-Sensitive

R:\\_REACTORS\\SO\\2007\\SO2007-13RP-GBM.wpd

RIV:SRI:DRP/C

RI:DRP/E

SRI:DRP/E

SRA:DRS

C:DRP/E

GBMiller

JEJosey

CCOsterholtz

DPLoveless

JAClark

/RA/

T-GBM

E=GBM

/RA/

/RA/

10/16 /07

10/17/07

10/16/07

10/17/07

10/19/07

OFFICIAL RECORD COPY

T=Telephone E=E-mail F=Fax

Enclosure

-1-

U.S. NUCLEAR REGULATORY COMMISSION

REGION IV

Docket:

50-361, 50-362

Licenses:

NPF-10, NPF-15

Report No.:

05000361/2007013; 05000362/2007013

Licensee:

Southern California Edison Co. (SCE)

Facility:

San Onofre Nuclear Generating Station, Units 2, 3

Location:

5000 S. Pacific Coast Hwy.

San Clemente, California

Dates:

June 27 through September 13, 2007

Inspectors:

J. Josey, Resident Inspector, Project Branch E, DRP

D. Loveless, Senior Reactor Analyst

G. Miller, Senior Resident Inspector, Project Branch C, DRP

C. Osterholtz, Senior Resident Inspector, Project Branch E, DRP

M. Sitek, Resident Inspector, Project Branch E, DRP

Approved By:

Jeffrey A. Clark, Chief

Project Branch E

Division of Reactor Projects

Enclosure

-2-

SUMMARY OF FINDINGS

IR 05000361/2007013, 05000362/2007013; 06/27/07 - 07/02/07; San Onofre Nuclear

Generating Station, Units 2, 3, and Independent Spent Fuel Storage Installation; Special

Inspection in response to an instrument air header break and Unit 2 trip on June 20, 2007.

The report covered a 6-day period (June 27 - July 2, 2007) of onsite inspection, with inoffice

review through September 13, 2007, by a special inspection team consisting of one senior

resident inspector, one resident inspector, and one senior reactor analyst. Eight findings were

identified. The significance of most findings is indicated by its color (Green, White, Yellow, or

Red) using Inspection Manual Chapter 0609, Significance Determination Process. Findings

for which the significance determination process does not apply may be Green or be assigned a

severity level after NRCs management review. The NRC's program for overseeing the safe

operation of commercial nuclear power reactors is described in NUREG-1649, Reactor

Oversight Process, Revision 3, dated July 2000.

Summary of Event

The NRC conducted a special inspection to better understand the circumstances surrounding

an instrument air header break and Unit 2 trip on June 20, 2007. In accordance with NRC

Management Directive 8.3, NRC Incident Investigation Program, it was determined that this

event involved multiple failures in systems used to mitigate the effects of an actual event,

involved potential adverse generic implications, and had sufficient risk significance to warrant a

special inspection.

A.

NRC-Identified and Self-Revealing Findings

Cornerstone: Initiating Events

Green. The inspectors reviewed a self-revealing Green finding involving

ineffective corrective actions taken in response to site and industry operating

experience with instrument air header ruptures. Specifically, contrary to

Section 6.2.3 of Procedure SO-123-I-1.42, Maintenance Division Experience

Report, Revision 0, the licensee failed to implement corrective actions to prevent

recurrence for an equipment failure with the potential to cause a significant plant

transient, and failed to appropriately consider previous industry and plant

experience similar to the event. Additionally, licensee personnel failed to properly

evaluate and take corrective actions based on industry operating experience

through 2006 involving improperly made soldered joints in instrument air systems.

As a result, an additional failure of an improperly made instrument air header joint

occurred at SONGS on June 20, 2007. The licensee entered this issue in their

corrective action program as Action Request AR 070600867.

This finding was more than minor since it was associated with the equipment

reliability attribute of the initiating events cornerstone and affected the cornerstone

objective to limit the likelihood of events that upset plant stability and challenge

critical safety functions. This finding required a Phase 2 analysis per the Manual

Chapter 0609, Significance Determination Process, Phase 1 Worksheets since

the loss of instrument air is a transient initiator resulting in the loss of the

feedwater system which is part of the power conversion system which can be used

to mitigate the consequences of an accident. Based on the results of the Phase 2

Enclosure

-3-

analysis and a subsequent Phase 3 analysis, the finding was determined to be of

very low safety significance (Green) because of the availability of the diverse

auxiliary feedwater system and the ability of the operators to depressurize the

steam generators and utilize the condensate system for heat removal. These

results were evaluated by a senior reactor analyst. This finding has a crosscutting

aspect in the area of problem identification and resolution associated with

operating experience in that the licensee failed to effectively implement changes to

station processes, procedures, and equipment in response to operating

experience involving improperly made instrument air system joints P.2(b).

(Section 2.1)

Green. The inspectors identified a Green noncited violation of Technical Specification 5.5.1.1 involving the failure to meet procedural requirements

following a loss of instrument air. Specifically, operators failed to monitor nitrogen

tank levels or take precautions for the possibility of oxygen-deficient areas in the

plant following actuation of the low pressure backup nitrogen system. The

licensee entered this issue in their corrective action program as Action

Request AR 070700291.

This finding was more than minor since it was associated with the human

performance attribute of the initiating events cornerstone and affected the

cornerstone objective to limit the likelihood of events that upset plant stability and

challenge critical safety functions. This finding required a Phase 2 analysis in

accordance with the Manual Chapter 0609, Significance Determination Process,

Phase 1 Worksheets since the loss of instrument air is a transient initiator resulting

in the loss of the feedwater system which is part of the power conversion system

which can be used to mitigate the consequences of an accident. Based on the

results of the Phase 2 analysis, the finding was determined to be of very low safety

significance because of the low likelihood of a complete loss of instrument air and

the availability of the auxiliary feedwater system. The cause of this finding has a

crosscutting aspect in the area of human performance associated with resources

because licensee personnel were not adequately trained on the operation of the

low pressure nitrogen system to effectively implement the abnormal operating

instruction H.2(b). (Section 2.2)

Cornerstone: Mitigating Systems

Green. A self-revealing, Green noncited violation of 10 CFR Part 50, Appendix B,

Criterion III, Design Control, was identified when Unit 2 experienced a loss of

instrument air due to the failure of a soldered joint. Specifically, the loss of

instrument air resulted in component cooling water (CCW) Pump 024 being in a

runout condition for approximately 75 minutes due to a previous system

modification. The licensee entered this issue in their corrective action program as

Action Requests AR 070700051 and 070600872.

This finding was greater than minor because it was associated with the mitigating

systems cornerstone attribute of design control and affected the associated

cornerstone objective to ensure the availability, reliability, and capability of systems

that respond to initiating events to prevent undesirable consequences. The finding

did not affect the initiating events cornerstone functions of the component cooling

water system because the condition would only have existed given a loss of

Enclosure

-4-

instrument air initiator had already occurred. In accordance with NRC Inspection

Manual Chapter 0609, Appendix A, Phase 1 Worksheet, Significance

Determination Process (SDP) Phase 1 Screening Worksheet for the Initiating

Events, Mitigating Systems, and Barriers Cornerstones, this finding was

determined to be of very low safety significance because the finding was a design

deficiency confirmed not to result in a loss of operability per Part 9900, Technical

Guidance, Operability Determination Process for Operability and Functional

Assessment. (Section 2.3)

Green. The inspectors reviewed a self-revealing Green finding involving the failure

to take effective corrective actions for a failed control room annunciator.

Specifically, after the annunciator for actuation of the backup nitrogen supply to

the instrument air system failed to function on demand on several occasions from

1994 through 2007, the corrective actions taken by the licensee to restore the

annunciator to service were inadequate and narrowly focused. The annunciator

subsequently failed to function during the loss of instrument air event on

June 20, 2007. The licensee entered this issue in their corrective action program

as Action Request AR 070601250.

This finding was more than minor since it was associated with the human

performance attribute of the initiating events cornerstone and affected the

cornerstone objective to limit the likelihood of events that upset plant stability and

challenge critical safety functions. This finding required a Phase 2 analysis in

accordance with the Manual Chapter 0609, Significance Determination Process,

Phase 1 Worksheets since the loss of instrument air is a transient initiator resulting

in the loss of the feedwater system which is part of the power conversion system

which can be used to mitigate the consequences of an accident. Based on the

results of the Phase 2 analysis, the finding was determined to be of very low safety

significance because of the low likelihood of a complete loss of instrument air and

the availability of the auxiliary feedwater system. This finding has a crosscutting

aspect in the area of problem identification and resolution associated with the

corrective action program in that the licensee failed to thoroughly evaluate the

failed annunciator such that the resolution appropriately addressed the causes

P.2(c). (Section 2.4)

Green. The inspectors identified a Green noncited violation of Technical Specification 5.5.1.1 involving the failure to maintain an adequate abnormal

operating instruction for a loss of instrument air event. The licensee entered this

issue in their corrective action program as Action Request AR 070801151.

This finding was more than minor because it was associated with the procedure

quality attribute of the mitigating systems cornerstone and affected the

cornerstone objective to ensure the availability, reliability and capability of systems

that respond to initiating events, in that a less than adequate abnormal operating

procedure could have prevented operators from promptly tripping the reactor,

allowing conditions to continue to degrade and resulting in a demand on the

reactor protection system. Using the Significance Determination Process Phase 1

Screening Worksheet in Appendix A of Inspection Manual Chapter 0609, the

inspectors determined this finding had very low safety significance because it did

not result in an actual loss of safety function per Part 9900, Technical Guidance,

Operability Determination Process for Operability and Functional Assessment.

Enclosure

-5-

This finding has a crosscutting aspect in the area of human performance

associated with resources in that the licensee failed to provide operators with

complete, accurate, and up-to-date procedures H.2(c). (Section 2.5)

Green. A self-revealing, Green noncited violation of 10 CFR Part 55.46(c)(1) was

identified involving the licensees failure to incorporate a design change in

modeling plant response for the plant-referenced simulator. Specifically, during

operator training in the plant-referenced simulator, the controlled bleedoff valves

for the reactor coolant pumps were modeled to fail closed on a loss of instrument

air, whereas the valves in the plant remained open during an actual loss of

instrument air event on June 20, 2007. The licensee entered this issue in their

corrective action program as Action Requests AR 070600873 and 070900160.

This finding was greater than minor because it was associated with the mitigating

systems cornerstone attribute of human performance and affected the associated

cornerstone objective to ensure the availability, reliability, and capability of systems

that respond to initiating events to prevent undesirable consequences. The

inspectors evaluated this finding using the Appendix I, Licensed Operator

Requalification Significance Determination Process worksheets of Manual

Chapter 0609 because the finding is a requalification training issue related to

simulator fidelity. The finding is of very low safety significance because the

discrepancy did not have an adverse impact on operator actions such that safety

related equipment was made inoperable during normal operations or in response

to a plant transient. This finding has a crosscutting aspect in the area of human

performance associated with resources in that the licensee did not provide

operators with adequate facilities and equipment for use in operator training

H.2(d). (Section 2.6)

Green. The inspectors identified a Green noncited violation of Technical Specification 5.5.1.1 involving the failure to meet procedural requirements

governing impaired annunciators. Specifically, after the identification of a failed

annunciator, operators did not enter the annunciator in the failed annunciator log

or mark the affected annunciator window with an annunciator compensatory action

flag. The licensee entered this issue in their corrective action program as Action

Request AR 070700291.

This finding was more than minor since it was associated with the human

performance attribute of the initiating events cornerstone and affected the

cornerstone objective to limit the likelihood of events that upset plant stability and

challenge critical safety functions. This finding required a Phase 2 analysis in

accordance with the Manual Chapter 0609, Significance Determination Process,

Phase 1 Worksheets since the loss of instrument air is a transient initiator resulting

in the loss of the feedwater system which is part of the power conversion system

which can be used to mitigate the consequences of an accident. Based on the

results of the Phase 2 analysis, the finding was determined to be of very low safety

significance because of the low likelihood of a complete loss of instrument air and

the availability of the auxiliary feedwater system. This finding has a crosscutting

aspect in the area of human performance associated with resources because the

operators were not sufficiently trained to consistently implement the annunciator

operating procedure H.2(b). (Section 2.7)

Enclosure

-6-

Green. A Green self-revealing finding was identified associated with the failure of

the reactor coolant pump controlled bleed off valve to shut during a loss of

instrument air event. The licensee failed to adequately implement corrective

actions from previously evaluated industry operating experience for new valve

regulators that were installed in the unit. The licensee entered this issue in their

corrective action program as Action Request AR 070600873.

The finding was greater than minor because it was associated with the mitigating

systems cornerstone attribute of design control and affected the associated

cornerstone objective to ensure the availability, reliability, and capability of systems

that respond to initiating events to prevent undesirable consequences. Using

Manual Chapter 0609, Significance Determination Process, Phase 1 Worksheet,

the finding is determined to have very low safety significance because the

condition only affected the mitigation systems cornerstone and it was confirmed

not to result in loss of operability per Part 9900, Technical guidance, Operability

Determination Process for Operability and Functionality Assessment

(Section 2.8).

B.

Licensee-Identified Violations

None.

Enclosure

-7-

REPORT DETAILS

1.0

SPECIAL INSPECTION SCOPE

The NRC conducted a special inspection at San Onofre Generating Station (SONGS) to

better understand the circumstances surrounding the loss of instrument air event on

June 20, 2007. On this occasion, instrument air pressure on Unit 2 dropped significantly

following the separation of a 3-inch air header in the auxiliary building. This caused the

feedwater control valves to stop functioning, resulting in an uncontrolled increase in

steam generator water level. Operators manually tripped the Unit 2 reactor. In

accordance with NRC Management Directive 8.3, it was determined that this event had

sufficient risk significance to warrant a special inspection.

The team used NRC Inspection Procedure 93812, Special Inspection Procedure, to

conduct the inspection. The special inspection team reviewed procedures, corrective

action documents, operator logs, design documentation, maintenance records, and

procurement records for the instrument air system. The team interviewed various

station personnel regarding the event. The team reviewed the licencees preliminary

root cause analysis report, past failure records, extent of condition evaluation,

immediate and long term corrective actions, and industry operating experience. A list of

specific documents reviewed is provided in Attachment 1. The charter for the special

inspection is included as Attachment 2.

1.1

Event Summary

During full power operation on June 20, 2007, a 3-inch diameter instrument air line failed

at an improperly soldered joint on the Unit 2 instrument air header. The joint completely

separated, resulting in a double-ended guillotine shear of the supply header and a

complete loss of instrument air to Unit 2. The loss of instrument air pressure caused the

feedwater control valves to stop functioning, and operators manually tripped the Unit 2

reactor as a result of an uncontrolled steam generator water level increase. Although

instrument air is a shared system at SONGS, a backup nitrogen system can support

system loads on the unaffected unit following a pipe break via excess flow check valves.

As a result, the pressure drop on Unit 3 was not as significant during the event and

operators maintained control of all functions.

Operators located the failed piping in the Unit 2 turbine building and were able to isolate

the break approximately thirty minutes after the event began. Operators applied a

temporary repair to the break and restored instrument air header pressure. Subsequent

investigations identified 32 additional leaking instrument air fittings in Unit 2 and Unit 3,

possibly as a result of improper joint fabrication during initial construction. Maintenance

personnel placed structural clamps on the leaking fittings to prevent additional piping

separations until permanent repairs could be made.

The time line below describes the major events following the separation of the

instrument air header fitting on June 20, 2007.

Enclosure

-8-

June 20, 2007

2244

Instrument air dryer Temp/Level/DP HI alarm received.

Control room instrument air header pressure noted to be 80 psig and lowering.

Instrument air pressure low alarm received on Unit 2. (90 psig setpoint)

Operators entered Procedure SO23-13-5, Loss of Instrument Air.

2245

Unit 2 air operated valves begin to move on their own.

Full Flow condensate polisher demineralizer bypass valves open.

Chemical volume control system letdown flow isolates.

Unit 3 instrument air pressure low alarm received. (90 psig setpoint)

2247

Steam Generator level noted to be 82% and rising in generator E088 on Unit 2.

Operators secured charging pumps due to loss of letdown and began manually

controlling pressurizer level.

Operators bypassed instrument air dryers. Indicated instrument air header

pressure in the control room increases from 42 psig to 67 psig.

2248

Heater drain pump P059 trips.

2250

Heater drain pump P058 trips.

E088 level approaching trip set point, manually tripped the Unit 2 reactor.

Entered Procedure SO23-12-1, Standard Post Trip Actions.

2252

Steam generator E088 level exceeds 100%.

2253

Operators manually tripped both main feed pumps.

2254

Operators initiated both trains of auxiliary feedwater. (EFAS)

Steam bypass control system responding sluggishly; both reactor temperature

and pressure slightly higher than expected. Operators begin controlling pressure

and temperature using one atmospheric dump valve.

2258

Steam generator E088 level returns to less than 100%.

2303

Entered Procedure SO23-12-2, Reactor Trip Recovery.

2321

Location of instrument air header rupture identified and isolated using manual

valves. Instrument air header pressure indicated in the control room immediately

recovers from 67 psig to 108 psig (normal operating pressure). Instrument air

dryer Temp/Level/DP HI and instrument air low pressure alarms clear.

Temporary repair (soft patch) put in place on the instrument air header.

2329

Component Cooling Water (CCW) Pump A noted to be in a runout condition,

operators started CCW Pump B.

0024

NRC notified of unit trip due to uncontrolled level rise in steam generator E088

upon loss of instrument air.

0030

Procedure SO23-12-1, Loss of Instrument Air, exited.

Enclosure

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1.2

Operator Response

The team assessed the response of the control room operators to the loss of instrument

air. The team reviewed operator logs, plant computer data, and strip charts to evaluate

operator performance in coping with the event and transient; verified that operator

actions were in accordance with the response required by plant procedures and training;

and verified that the licensee identified and implemented appropriate corrective actions

associated with personnel performance problems that occurred during the event. The

team also conducted interviews with each of the control room operators who were on

shift the night of the event.

The team concluded the operators acted appropriately to manually trip the Unit 2 reactor

and turbine and place the unit in a safe condition. The inspectors also concluded the

operators acted promptly and appropriately in recovering the instrument air system and

in maintaining Unit 3 at power. However, the team also identified several opportunities

for improvement in some aspects of operator response and training associated with the

event.

Through interviews with control room personnel, the inspectors noted a general

weakness in the operators understanding of the design and integrated operation of the

instrument air and low pressure nitrogen systems. As an example, several operators

erroneously stated that the respiratory/service air system was supporting the Unit 3

instrument air loads during the event, when in fact the Unit 3 loads were being supplied

by the backup nitrogen system. Several operators also believed their efforts to bypass

the instrument air filters and to place an additional dryer in service had a positive effect

on restoring instrument air pressure to Unit 2, when in reality the Unit 2 instrument air

header pressure was not recoverable due to the complete separation of the pipe header

from the supply lines.

The inspectors concluded the operators understanding of the event on June 20, and

their ability to diagnose and respond to future events involving a loss of instrument air,

were complicated by the sparse control room instrumentation provided for the

instrument air system. Specifically, operators in both control rooms are provided with

one indication each for respiratory/service air supply pressure, backup nitrogen system

supply pressure, and instrument air supply pressure. There are no indications for actual

air header pressure at the system loads for either Unit 2 or Unit 3. Additionally, the

control room indications provided real-time pressure indication only; there were no strip

charts recorders to allow prompt diagnosis of pressure trends, nor were there any

computer points available to provide pressure indication, tracking, or trending

information to the control room operators.

The inspectors reviewed Procedure SO23-13-5, Loss of Instrument Air, Revision 5,

which was the abnormal operating instruction used by the operators to respond to the

loss of instrument air pressure on June 20, 2007. The inspectors concluded that given

the limited data available to plant operators in the control rooms, the abnormal operating

instruction did not provide sufficient guidance to ensure operators would be able to take

prompt action to mitigate the effects of a loss of instrument air in all circumstances. The

inspectors determined the failure to maintain an adequate operating instruction to

respond to a loss of instrument air was a violation of Technical Specification 5.5.1.1.

This finding is described further in Section 2.5 of this report.

Enclosure

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Through review of operator logs, the marked-up copy of the abnormal operating

instruction for loss of instrument air used during the event, and interviews of operators,

the inspectors identified that operators had failed to take the required actions specified

in the abnormal operating instruction for actuation of the backup nitrogen system.

Specifically, the operators did not take steps to monitor for oxygen-deficient areas of the

plant caused by nitrogen leakage from the instrument air system and did not begin

monitoring nitrogen tank levels. The inspectors also noted that control room

Annunciator 61B38, N2 SUPPLY TO INST AIR HEADER ON, failed to alarm during

the event, which, when combined with the aforementioned weak operator understanding

of the system and limited control room instrumentation, likely contributed to the

operators failure to take the actions of the abnormal operating instruction. The

inspectors noted the failure to take these actions had the potential to result in operator

injury or death from entering oxygen-deficient areas in the plant. The inspectors

determined the failure to follow the requirements of the abnormal operating instruction

was a violation of Technical Specification 5.5.1.1. This finding is discussed further in

Section 2.2 of this report.

The inspectors examined the post-trip review package assembled by the licensee

following the trip of Unit 2. The inspectors noted the post-trip review package

appropriately addressed the response and operation of safety-related plant equipment

to the event. The post-trip review also properly identified operator performance issues

associated with a missed surveillance requirement and implemented appropriate

corrective actions. The inspectors concluded the licensees post-trip review was

adequate per the guidance of Generic Letter 83-28, Required Actions Based on

Generic Implications of Salem ATWS Events. However, the inspectors identified some

weaknesses in the scope and thoroughness of the review in regard to the nonsafety-

related aspects of the event. For example, the post trip review did not identify the failure

of Annunciator 61B38 to alarm as mentioned above and described further in Section 1.4

of this report. The review package also contained a typographical error identified by the

inspectors that, had the recorded value been correct, would have indicated that the

reactor trip circuit breakers had failed to open within their design time limit. The review

also did not address the weaknesses in operator understanding of the event or the

failure of operators to follow the requirements of the abnormal operating instruction for

actuation of the backup nitrogen system as described above.

The licensee initiated a root cause evaluation to assess the above issues related to the

operator response and post-trip review for the June 20, 2007, loss of instrument air

event as part of Action Request AR 070700291.

1.3

Instrument Air System Interactions

The instrument air system at SONGS consists of three motor driven instrument air

compressors, two parallel air dryers and four parallel air filters, all of which are located in

the turbine building. Backup pressure sources for instrument air are provided by the low

pressure nitrogen system and the respiratory/service air system. The instrument air

system is designed to provide a continuous supply of filtered, dried, and essentially oil-

free air for pneumatic instruments and valves in both units.

During normal system operation, one of the compressors is in continuous operation

while the other two compressors are in standby. The standby compressors will start and

stop automatically as required to supplement the running compressor to meet system

Enclosure

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demand. The instrument air header is divided between the two units by check valves

installed in the supply headers and in the unit crossover header in the radwaste building.

Non-safety related nitrogen supply lines with isolating valves and excess flow check

valves are located downstream of the unit check valves in the air supply lines to provide

a backup nitrogen supply for each units instrument air header. The excess flow check

valves isolate on high flow, which prevents a failure in one units air piping from causing

an excessive instrument air pressure drop in the other unit. A second backup supply for

the instrument air system is provided by the respiratory/service air system. The

respiratory/service air system is connected to the instrument air supply lines upstream of

the instrument air dryers.

The instrument air system supplies the motive force to all pneumatically operated valves

and instruments in both units. All pneumatically operated valves are designed to fail to

their safe position on a loss of instrument air. Pneumatic valves with a safety function

are described in Table 9.3-1 of the SONGS Final Safety Analysis Report (FSAR) and

include: saltwater cooling system isolation valves and lubrication valves, component

cooling water isolation valves, shutdown cooling heat exchanger isolation valves, safety

injection line check valve leakoff line isolation valves, safety injection tank fill and drain

lines, and auxiliary feedwater pump steam supply valves. Significant non-safety related

pneumatic valves include the chemical volume control system letdown isolation valves,

pressurizer normal spray valves, main feedwater regulating valves, steam bypass

control system valves, reactor coolant pump seal controlled bleedoff isolation valves,

and component cooling water noncritical loop isolation valves.

1.4

Plant Response

The inspectors reviewed operator logs, alarm history, and available trend information to

evaluate the plant response to the loss of instrument air header pressure to ensure that

all systems responded as designed. The inspectors concluded the instrument air

system functioned as described in the FSAR. Following the break in the Unit 2 air

header, the excess flow check valve in the backup nitrogen supply line to Unit 2 closed

to isolate the break and successfully mitigated the effect of the transient on Unit 3 as

designed. The inspectors also concluded the integrated plant response to the overall

transient also occurred as described in the FSAR, with some exceptions as noted below.

In the post trip review package, the licensee noted excessive flow existed in the

component cooling water (CCW) system for approximately 75 minutes following the

event, which placed the CCW Pump A in a runout condition. The excess system flow

resulted when the shutdown cooling heat exchanger isolation valve failed open as

designed on the loss of instrument air pressure. Although in the original plant design

the CCW noncritical loop isolation valves failed shut on a loss of instrument air pressure

to isolate the shutdown cooling heat exchanger from the system, the licensee installed a

modification in 1995 to allow the noncritical loop isolation valves to remain open in order

to maintain cooling water for the reactor coolant pumps. Consequently, the opening of

the shutdown cooling heat exchanger isolation valve placed an additional load on the

system in excess of the capacity of the operating CCW pump. The inspectors

determined this was a violation of 10 CFR Part 50, Appendix B, Criterion III, Design

Control. This finding is discussed further in Section 2.3 of this report.

In the post-trip review package and during interviews with the inspectors, the operators

noted the controlled bleed off valve for the reactor coolant pump seals remained open

Enclosure

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following the loss of instrument air. During interviews with the inspectors, the operators

stated that in operator training in the site simulator, the CBO valve always failed shut on

a loss of instrument air pressure, requiring the operators to trip the reactor coolant

pumps to ensure the integrity of the reactor coolant pump seals. As a result, when the

CBO valve indicated open during the event on June 20, 2007, control room operators

requested local, independent verification of the actual position of the CBO valve. The

inspectors concluded the discrepancy between actual plant response and that modeled

in the simulator negatively impacted operator response to the loss of instrument air

event. The inspectors determined this simulator fidelity issue was a violation of 10 CFR Part 55.46. This finding is discussed further in Section 2.6 of this report.

In reviewing the cause for the failure of the CBO valve to close on the loss of instrument

air pressure, the licensee determined that the regulator for the valve had been replaced

with a new style regulator in February 2004. The new style regulator was installed

because the original model had become obsolete. Whereas air pressure would leak off

the original model regulator causing the associated valve to close on a loss of

instrument air, the new regulator contained improved seals that locked in air pressure

and allowed the associated valve to remain open. Although the licensees substitution

equivalency evaluation required a design change impact review prior to installing the

new model regulators in the plant, the engineers performing the impact review for the

CBO valve failed to review the FSAR and so did not identify that the CBO valves were

designed to fail closed on a loss of instrument air. A finding associated with the failure

to perform an adequate design change impact review is discussed further in Section 2.8

of this report.

During the loss of instrument air event, Annunciator 61B38, N2 SUPPLY TO INST AIR

HEADER ON, failed to alarm, complicating operating understanding of and response to

the event as described in Section 1.2 of this report. The licensee initiated Action

Request AR 070601250 to address the failed annunciator. While in the control room

three days later, the inspectors noticed there were no labels, warning flags, or other

devices affixed to or logged for the nonfunctional annunciator. The inspectors noted

that should a similar loss of instrument air pressure event recur, the absence of any

warning labels or other devices to alert operators to the nonfunctional annunciator could

cause the operators to fail to take the appropriate steps per the annunciator response

instruction and loss of instrument air abnormal operating instruction to monitor enclosed

spaces for oxygen concentration and monitor the nitrogen tank levels. Due to

instrument air system leakage, actuation of the backup nitrogen system without the

compensatory action of monitoring enclosed spaces for oxygen concentration could

potentially result in operator injury or death from entering oxygen-deficient areas of the

plant. This inspectors determined the failure to appropriately track the nonfunctional

control room annunciator was a violation of Technical Specification 5.5.1.1. This finding

is discussed further in Section 2.7 of this report.

1.5

Root Cause Evaluation

The inspectors reviewed the accuracy and thoroughness of the licensee cause

determination as described in the root cause evaluation, Unit 2 Instrument Air Soldered

Joint Failure, performed as part of Action Request AR 070600867. The licensees root

cause evaluation used events and causal factors analysis and failure modes and effects

Enclosure

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analysis to evaluate the physical piping failure, the use of operating experience at the

site, and the implementation of the preventive maintenance program in the instrument

air system.

For the physical piping failure, the licensee performed a metallurgical analysis of the

failed joint. The analysis showed the original solder coverage within the joint was less

than 30% of the joint interface. Corrosion facilitated by residual flux in the joint

weakened the solder over time until the eventual failure of the fitting. The licensee

concluded the cause for the improper solder coverage was an improper fit up causing

an excessive gap in the joint due to poor workmanship during initial construction. The

analysis concluded the cause of the poor workmanship was a lack of supervisory

monitoring and reinforcement, and the root cause of the physical joint failure was a lack

of intrusive testing and inspections of the instrument air system during initial

construction. The analysis did not identify corrective actions specific to the identified

causes since the events examined occurred during initial construction. Corrective

actions were identified to develop an inspection plan to locate additional leaking joints

and to periodically inspect the clamps installed on improperly made joints until repairs

can be made.

The root cause analysis also examined the ineffective review and use of industry

operating experience (OE) at the site to determine why the event had not been

prevented despite the existence of sufficient OE to foresee its occurrence. The licensee

concluded the ineffective use of OE was the result of an inappropriate cultural bias in

the engineering department that led engineers to review OE from a defensive

standpoint; i.e., the goal of the engineers performing reviews was to determine why a

particular OE was not applicable to the station. The licensee determined this culture

was reinforced by insufficient site expectations for OE procedural use and

documentation. The licensee developed corrective actions to strengthen site standards

and expectations for OE procedure use and documentation and to perform

benchmarking among industry peers to incorporate best practices for OE use.

The final portion of the licensees root cause evaluation examined the lack of an

adequate preventive maintenance program for the instrument air check valves and the

backup nitrogen flow indication switch. The licensee concluded the apparent cause for

the lack of preventive maintenance tasks was ineffective supervisory monitoring. The

licensee developed corrective actions to reinforce expectations for supervisory

performance and to implement preventive maintenance tasks for the instrument air

check valves.

The inspectors reviewed the licensees root cause evaluation and determined the

metallurgical analysis and cause evaluation for the physical piping failure was thorough

and technically sound. However, the inspectors concluded that the root cause

evaluation as a whole was narrowly focused and in some cases lacked specific,

comprehensive corrective actions.

The inspectors considered the evaluation to be narrowly focused since it did not fully

address all the factors and behaviors that contributed to the nature, magnitude and

timing of the event. For example, the evaluation did not discuss in detail a precursor

event in the form of a failed thermowell fitting in the instrument air system that occurred

in 1994. The evaluation also failed to address the poor quality of the OE review

performed in 1992. The extent of condition review made only a passing reference to the

Enclosure

-14-

domestic water system and did not contain a complete discussion of systems potentially

affected by the identified root cause. Additionally, the maintenance review in the root

cause evaluation did not discuss the scoping or performance of the instrument air

system under the Maintenance Rule (10 CFR Part 50.65). Also, the extent of cause

review for the failed joint noted that site engineers had not appropriately addressed the

instrument air system under the station Equipment Reliability Improvement Program, but

the report did not appear to investigate why that had happened or whether there were

potentially other systems that may have been similarly overlooked.

The inspectors noted that the narrow focus of the report was also reflected in the

assignment of corrective actions. Specifically, the licensee identified poor supervisory

monitoring and oversight as an apparent cause for the improperly soldered joint, but

identified no corrective actions due to the age of the issue. However, later in the same

report, the licensee identified poor supervisory monitoring and oversight as an apparent

cause for the failure to establish adequate preventive maintenance tasks for instrument

air system. Corrective actions in this case to reinforce standards and improve

performance were directed only to the engineering organization.

The inspectors noted that in some cases, the causes identified in the root cause

evaluation tended to be associated with a single, broad corrective action such as

strengthen site standards. While the inspectors did not disagree with the intent of the

corrective action, the generalized language leaves the method of implementation open

to interpretation and complicates the ability of the stations assessment organization to

perform effectiveness reviews. In these cases, the inspectors concluded a set of

specific, focused, and measurable corrective actions may have been more appropriate.

1.6

Event Precursors

The team performed a search of corrective action program databases to identify

previous instrument air system piping problems that may have been precursors to the

event on June 20, 2007. The inspectors identified the potential event precursors

described below.

The inspectors noted that in June 1994, both Units 2 and 3 experienced a loss of

instrument air event due to the failure of a soldered joint retaining a threaded thermowell

attachment to the instrument air header. In the failure analysis for the fitting, the

licensee determined the cause of the separation was poor quality workmanship that

occurred during original installation. The licensee determined that when the fitting was

initially installed, it was not centered, causing an excessive gap on one side of the joint

and resulting in inadequate solder penetration. The licensee also identified that the joint

was designed to be silver brazed per the manufacturers specification and should not

have been soldered, and that this joint had most likely been leaking since original

installation since a portion of the pipe joint had no filler metal in it. Although this event

did not result in a reactor trip, the inspectors noted the cause and nature of the failure

were nearly identical to that experienced on June 20, 2007.

In April, 2007, both Unit 2 and Unit 3 experienced a loss of instrument air event due to a

trip of the running air compressors. During this event as well as during the June 1994

loss of instrument air event described above, the annunciator for actuation of the

backup nitrogen supply to the instrument air system failed to alarm in the control room.

Following the annunciator failure in 1994, licensee maintenance technicians noted that

Enclosure

-15-

the limit switch was dirty. Since a replacement limit switch was not available, the

technicians cleaned the installed limit switch and returned it to service. In April 2007,

licensee maintenance technicians noted that the travel on the switch was satisfactory

and there were no problems on the electrical part of the system. No other work was

documented. During the event on June 20, 2007, the annunciator for actuation of the

backup nitrogen system again failed to alarm in the control room. Although the

April 2007 event was caused by a compressor failure and did not result in a reactor trip,

the inspectors noted the plant response, particularly as it related to the flow switch for

actuation of the backup nitrogen system, was similar to the event on June 20, 2007. A

finding associated with the failure of the licensee to take effective corrective actions for

the nitrogen system flow switch is described in Section 2.4 of this report.

1.7

Instrument Air System Maintenance and Testing

The inspectors reviewed the licensees program for maintenance and inspection of the

instrument air system, particularly as it related to the historical health of the instrument

air compressors and piping system.

The inspectors noted the performance of the instrument air system was monitored

under performance criteria established per the guidance for Category a(2) systems

under the Maintenance Rule. During discussions with the system engineer and site

Maintenance Rule coordinator, the inspectors learned the system was under

consideration for goal setting and monitoring per Category a(1) of the Maintenance

Rule. The licensee subsequently established goals and began monitoring the

performance of the instrument air system per Category a(1). The team considered this

action appropriate. The team also noted there had been several functional failures of

the three instrument air compressors over the past two years, and at one point earlier in

the year a temporary air compressor was installed to supplement the existing instrument

air compressors. The team noted this situation was nearly identical to that described in

NRC Inspection Report 50-361:362/97-22 as indicative of poor performance requiring

the goal setting and monitoring per Category a(1) of the Maintenance Rule. Given this

operating history, the team concluded it may have been appropriate for the station to

have classified the instrument air system as Category a(1) much earlier in the year.

However, the inspectors noted that such classification would have had no impact on the

prevention or mitigation of the loss of instrument air event experienced at the station on

June 20, 2007.

The inspectors also examined maintenance work orders for individual components in the

instrument air and low pressure nitrogen systems. The inspectors noted that no

preventive maintenance actions existed for the excess flow check valves in the supply

header for backup nitrogen to the instrument air system. The inspectors considered this

inappropriate given these valves have a function credited in the FSAR to prevent a

break in one units instrument air header from causing a loss of instrument air to the

other unit. Since check valves can not be considered inherently reliable components,

the inspectors concluded the licensee had failed to perform adequate preventive

maintenance to ensure the excess flow check valves would perform their intended

function. The inspectors determined this was a violation of 10 CFR Part 50.65a(2).

However, since the excess flow check valves did perform their intended function during

the actual loss of instrument air event on June 20, 2007, the inspectors considered this

Enclosure

-16-

violation to be minor. The licensee entered this violation in their corrective action

program as Action Requests AR 070600867 and AR 070900333, and evaluated the lack

of preventive maintenance items in the instrument air system as part of the root cause

evaluation for the loss of instrument air event.

1.8

Industry Operating Experience (OE) and Potential Generic Issues

The inspectors performed searches of operating experience databases and other

sources to identify reports of similar problems, both inside and outside the nuclear

industry.

During the late 1980s and early 1990s, a significant amount of Operating

Experience (OE) identified instances where facilities had experienced transients and/or

trips due to failures of soldered joints in instrument air system piping due to poor

workmanship during initial construction. The licensee documented their review of the

industry OE in their corrective action program (CAP) as Independent Safety

Engineering Group Operating Experience Evaluation, dated January 22, 1992. In this

review, the licensee evaluated the identified causes and corrective actions from the OE

and determined that soldering at SONGS was loosely controlled and better training was

necessary for welders at the facility. However, the licensee asserted in their evaluation

that failures due to inadequate fit-up or solder penetration typically occur within a

relatively short time frame after startup. The licensee concluded that since the

instrument air system had been in service for many years at SONGS and no significant

problems had yet been identified, then no corrective actions were necessary with

respect to the installed instrument configuration. The inspectors considered this

conclusion to be without a valid technical basis. A finding associated with this evaluation

is discussed in Section 2.1 of this report.

In addition to the internal site experience described above and in Section 1.6 of this

report, the inspectors identified additional OE in the form of Licensee Event Reports

(LERs). Most notably, the inspectors reviewed LER 05000336/2006-002-00, Manual Reactor Trip Due to Trip of Both Feed Pumps Following a Loss of Instrument Air,

April 21, 2006, and LER 05000440/2006-005-00, Decreasing Instrument Air Pressure

Results in Manual Reactor Protection System Actuation, February 9, 2007. Both

reports describe reactor trips brought about by instrument air header joint separation. In

both cases, the cause of the header joint separation was inadequate workmanship

during initial construction. Though the site OE coordinator indicated the licensee

reviewed all Licensee Event Reports for applicability to SONGS, the inspectors did not

identify any documents in the licensees corrective action program that evaluated these

events. The inspectors determined the lack of documentation in the CAP indicated the

site OE organization had determined the above described events were not applicable to

SONGS. The inspectors concluded the licensee had missed multiple opportunities both

historically and recently to identify the vulnerability presented by improperly made joints

in the instrument air system.

Given the failure history described above, the inspectors concluded the construction

methods and controls in place during initial construction at SONGS were not unique.

Therefore, the potential for separation of instrument air piping due to improperly made

joints represents a potential generic concern for all facilities with instrument air systems

utilizing soldered joints in copper piping headers.

Enclosure

-17-

2.0

SPECIAL INSPECTION FINDINGS

2.1

Ineffective Corrective Actions for Instrument Air Header Ruptures

The inspectors reviewed a self-revealing Green finding involving ineffective corrective

actions taken in response to site and industry operating experience with instrument air

header ruptures. Specifically, contrary to Section 6.2.3 of Procedure SO-123-I-1.42,

Maintenance Division Experience Report, Revision 0, the licensee failed to implement

corrective actions to prevent recurrence for an equipment failure with the potential to

cause a significant plant transient, and failed to appropriately consider previous industry

and plant experience similar to the event. Additionally, licensee personnel failed to

properly evaluate and take corrective actions based on industry operating experience

through 2006 involving improperly made soldered joints in instrument air systems. As a

result, an additional failure of an improperly made instrument air header joint occurred at

SONGS on June 20, 2007.

On June 20, 2007, both Units 2 and 3 experienced a loss of instrument air event due to

the failure of a three-inch instrument air line header fitting. As a result of the break

location, a loss of manual feedwater control occurred on Unit 2 which ultimately resulted

in a manual reactor trip due to high steam generator level.

The licensee performed a Root Cause Evaluation of this event, as documented in Action

Request AR 070600867. The licensee also performed a metallurgical analysis of the

failed joint as documented in SONGS Unit 2 Instrument Air System Failed Fitting

Metallurgical Evaluation, dated June 27, 2007. During these evaluations, the licensee

determined the root cause of the event to be poor workmanship of the header joint

during initial installation. The licensees metallurgical analysis also concluded the fitting

had only thirty percent solder coverage within the joint and had likely been leaking air

since the plants first operating cycle. Subsequent investigations by the licensee

identified 32 additional joints leaking air in the instrument air headers of both units. The

licensee installed temporary structural clamps on the leaking fittings tp prevent

additional separations until permanent repairs could be made.

The inspectors reviewed the licensees root cause evaluation and metallurgical analysis

for this event. During their review of the issue, the inspectors noted that there had been

a previous similar air header failure at SONGS, and that the licensee had previously

evaluated related industry Operating Experience (OE) involving issues with soldered

joints.

During the late 1980s and early 1990s, a significant amount of Operating Experience

(OE) identified instances where facilities had experienced transients and/or trips due to

failures of soldered joints in instrument air system piping. The identified failures were

due to a lack of adequate controls during the initial makeup of soldered joints.

Specifically, inadequate fit-up of the joints or inadequate solder penetration were

identified as the causes of the failures. The licensee performed a review documented in

Independent Safety Engineering Group Operating Experience Evaluation, dated

January 22, 1992, to evaluate applicability of the OE to the facility. In this review, the

licensee evaluated the identified causes and corrective actions from the OE and

determined that soldering at SONGS was loosely controlled and better training was

necessary for welders at the facility. However, the licensee asserted in the evaluation

that any failures due to inadequate fit-up or solder penetration would typically have

Enclosure

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occurred within a relatively short time frame after startup. The licensee concluded that

since the instrument air system had been in service for many years and no significant

problems had yet been identified, then no corrective actions were necessary with

respect to the installed instrument air configuration.

In June 1994, both Units 2 and 3 experienced a loss of instrument air event. The

licensee investigated the cause and determined it was due to the failure of a soldered

joint retaining a threaded attachment, a Brazolet fitting, to the air header. The Brazolet

fitting was being used for a thermowell in the instrument air header. The licensee

performed a failure analysis of the fitting documented in Failure Analysis Report

No.94-006, dated July 8, 1994, to determine the cause of the joint failure. During this

analysis, the licensee determined the cause of the soldered fitting failure was poor

quality workmanship that occurred during original installation. The licensee determined

that when the fitting was initially installed, it was not centered, but rather cocked to one

side. This was not as required by the procedure and resulted in an excessive gap on

one side of the joint. This gap deprived one side of the joint of filler material, resulting in

inadequate solder penetration. The licensee also identified that the joint was designed

to be silver brazed per the manufacturers specification and should not have been

soldered.

Based on the metallurgical analysis, the licensee determined that the joint failure in

July 1994 was due to fatigue cracking that originated at the area between the soldered

and un-soldered sections of the joint. The failure analysis also identified that this joint

had most likely been leaking since installation. This was based on the fact that a portion

of the pipe joint had no filler metal in it. Since the joint was located approximately ten

feet off the floor in a high noise area, the leakage had not been previously identified.

The failure analysis also recommended that to prevent recurrence, all brazolet fittings in

the instrument air system should be examined both for leaks and for use of solder. The

analysis further identified that properly soldered joints fittings should be able to tolerate

instrument air header pressure indefinitely; however, if leaks were found, the fittings

should be replaced using silver braze at the earliest opportunity.

The inspectors concluded the licensees evaluation of OE performed in 1992 was

inadequate in that it improperly determined that failures due to inadequate fit-up and/or

inadequate solder penetration would have occurred within a relatively short time frame.

The inspectors also determined that the licensee failed to adequately reassess this

position following the instrument air line joint failure in 1994. The inspectors noted that

as recently as 2006, the licensee had inappropriately screened additional industry OE

relating to the failure of inadequately made instrument air piping joints as not applicable

to the station. The inspectors concluded the licensee failed to take effective corrective

actions for inadequately made joints in the instrument air system since the corrective

actions for the 1994 event and in response to industry OE were narrowly focused on

soldered Brazolet fittings and failed to evaluate soldered joints as a whole.

The safety significance and enforcement aspects of this finding are described in

Sections 3.1 and 4.1, respectively.

2.2

Failure to Follow Abnormal Operating Instruction for the Loss of Instrument Air

The inspectors identified a Green noncited violation of Technical Specification 5.5.1.1

involving the failure to meet procedural requirements following a loss of instrument air.

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Specifically, operators failed to monitor nitrogen tank levels or take precautions for the

possibility of oxygen-deficient areas in the plant following actuation of the low pressure

backup nitrogen system.

The instrument air system at SONGS utilizes a low pressure nitrogen system as a

backup pressure source. An instrument air system pressure drop below 83 psig will

automatically actuate a control valve in the nitrogen system to supplement the

instrument air from liquid nitrogen storage tanks. A flow switch downstream of the

control valve is designed to provide an annunciator in the control when the nitrogen

system is actuated. While the air systems are being supplied by nitrogen, normal

system leakage can result in oxygen-deficient areas in enclosed spaces of the plant,

and the liquid nitrogen tank levels will decrease more rapidly than usual from the

addition of the instrument air loads. The nitrogen supply lines are provided with isolating

check valves and excess flow check valves to prevent a failure in one units piping from

causing an excessive pressure drop in the other unit.

On June 20, 2007, an instrument air header ruptured in Unit 2. Although the low

pressure nitrogen system functioned as designed to provide nitrogen to the Unit 3 air

header, the control room annunciator for nitrogen system actuation did not alarm. The

instrument air header low pressure alarms did actuate on both units, and control room

operators began taking required actions per Procedure SO23-13-5, Loss of Instrument

Air, Revision 5. Although a step in the procedure directed operators to monitor nitrogen

tank levels and monitor for oxygen concentrations in enclosed spaces following nitrogen

system actuation, this step was not performed. The inspectors noted the failure to take

these actions had the potential to result in a Unit 3 trip from nitrogen tank depletion or

the injury or death of personnel from entry into oxygen-deficient spaces.

During interviews with the inspectors, several control room operators demonstrated

knowledge weaknesses related to the operation of the backup pressure sources for

instrument air. For example, several operators mistakenly stated the Unit 3 air header

pressure had been supplied by the respiratory/service air system during the event. The

inspectors concluded that although the failed annunciator likely contributed to the

operators confusion, the failure to perform the required actions of the abnormal

operating instruction resulted from the operators poor understanding of the operation of

the nitrogen backup to the instrument air system.

The safety significance and enforcement aspects of this finding are described in

Sections 3.2 and 4.2, respectively.

2.3

Inadequate Evaluation Results in Runout of Component Cooling Water Pump

A self-revealing, Green noncited violation of 10 CFR Part 50, Appendix B, Criterion III,

Design Control, was identified when Unit 2 experienced a loss of instrument air due to

the failure of a soldered joint. Specifically, the loss of instrument air resulted in

component cooling water (CCW) Pump 024 being in a runout condition for

approximately 75 minutes due to a previous system modification.

In 1995, the licensee implemented a design change to the CCW system to provide

backup nitrogen to the non-critical loop (NCL) supply and return isolation valves. The

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design change was made to ensure that CCW flow would be maintained to the reactor

coolant pump (RCP) seals during a loss of instrument air event. This would preclude

the licensee from the need to secure the RCPs due to a loss of CCW cooling in the

event of a loss of instrument air pressure.

On June 20, 2007, the CCW system was aligned with the Train A Pump 024 in

operation with a normal full operating load on the system, including the non-critical loop.

The Train B pump was in standby. At approximately 10:45 pm, Unit 2 experienced a

loss of instrument air when a 3-inch air header fitting separated in the auxiliary building.

Following the loss of instrument air pressure, the shutdown cooling heat exchanger

isolation valves failed opened as designed. Since the NCL isolation valves remained

open, the increased system load from the shutdown cooling heat exchanger caused the

CCW pump flow rate to increase to approximately 300 gallons per minute more than its

maximum design flow limit of 16,000 gallons per minute, placing the pump in a runout

condition. The pump operated in this condition for approximately 75 minutes before

operators took action to reduce system flow rate.

The inspectors reviewed this issue and determined that the licensee had not performed

an adequate hydraulic analysis of the CCW system in 1995 when implementing the

design change to maintain the NCL supply and return isolation valves open following a

loss of instrument air. The inspectors determined that this design change directly

contributed to placing the CCW pump in a runout condition following the loss of

instrument air.

The safety significance and enforcement aspects of this finding are described in

Sections 3.3 and 4.3, respectively.

2.4

Ineffective Corrective Actions for a Failed Control Room Annunciator

The inspectors reviewed a self-revealing Green finding involving the failure to take

effective corrective actions for a failed control room annunciator. Specifically, after the

annunciator for actuation of the backup nitrogen supply to the instrument air system

failed to function on demand on several occasions from 1994 through 2007, the

corrective actions taken by the licensee to restore the annunciator to service were

inadequate and narrowly focused. The annunciator subsequently failed to function

during the loss of instrument air event on June 20, 2007.

In June 1994, SONGS Units 2 and 3 experienced a loss of instrument air event during

which the annunciator for actuation of the backup nitrogen supply to the instrument air

system failed to actuate in the control room. The licensee entered this into their

corrective action program and generated Maintenance Order 94062628000 to

investigate and correct the issue. During the investigation, licensee maintenance

technicians noted that the limit switch was dirty. Since a replacement limit switch was

not available, the licensee cleaned the installed limit switch and returned it to service.

The work order subsequently closed with no further actions taken by the licensee.

While the licensee was performing an evolution to repressurize the backup nitrogen line

to the instrument air system in May 1996, the annunciator for actuation of the backup

nitrogen supply to instrument air again failed to actuate in the control room. The

licensee entered this event into their corrective action program as Action Request

AR 960500111. In this AR the licensee determined that possible causes of the failure

Enclosure

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were slow flow rate, not enough to flow to open the check valve far enough to trip the

limit switch, or the possibility of a problem with the limit switch. The licensee generated

Maintenance Order 94062628001 to investigate and correct the issue. During their

inspection, the licensee maintenance technicians found rust on the limit switch and

determined this to be the cause of the failure. The limit switch was replaced, and the

licensee verified that it worked electrically. The inspectors noted the maintenance order

called for an operational test of the limit switch, but none was performed.

In April 2007, Units 2 and 3 experienced a loss of instrument air event. During this

event, the annunciator for actuation of the backup nitrogen supply to the instrument air

system again failed to actuate in the control room. The licensee entered this into their

corrective action program as AR 070400776 and generated Maintenance Order

07041277000 to investigate and correct the issue. During their inspection, the licensee

maintenance technicians noted that the travel on the switch was satisfactory and there

were no problems on the electrical part of the system. No other work was documented.

On June 20, 2007, both Unit 2 and Unit 3 experienced a loss of instrument air pressure

due to the failure of a three-inch instrument air line header fitting. During this event, the

annunciator for actuation of the backup nitrogen supply to the instrument air system

failed to actuate in the control room again. The licensee entered this into their corrective

action program as AR 070601250.

The inspectors concluded that the licensee failed to adequately evaluate and correct the

issue associated with the limit switch. During their review, the inspectors also noted that

the licensee had not questioned or investigated the operational aspects of the limit

switch. Instead, the licensee had narrowly focused on testing only the electrical portion

of the system. The inspectors determined that the licensee had not operationally tested

the limit switch during any of their corrective actions.

The licensee subsequently performed an operational test of the limit switch. During this

testing, the licensee determined the nitrogen flow through the check valve was not

sufficient to actuate the limit switch. Consequently, the limit switch would never have

functioned to actuate its associated control room annunciator. The licensee entered this

issue into their corrective action program.

The safety significance and enforcement aspects of this finding are described in

Sections 3.4 and 4.4, respectively.

2.5

Inadequate Procedure for a Loss of Instrument Air

The inspectors identified a Green noncited violation of Technical Specification 5.5.1.1

involving the failure to maintain an adequate abnormal operating instruction for a loss of

instrument air event.

Procedure SO23-13-5, Loss of Instrument Air, Revision 5, specifies operator actions to

mitigate the effects of excessive instrument air system leakage or the loss of the

instrument air compressors. The inspectors reviewed the procedure and noted the

following:

Step 1.a of the procedure was followed by a caution stating:

Enclosure

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A large break downstream of the nitrogen supply may cause the nitrogen

excess flow check valve to seat. This may be indicated by falling nitrogen

header pressure on 2/3PI-5344B, followed by rapid return to > 80 psig.

The inspectors noted the nitrogen header pressure indication on 2/3PI-5344B

was not provided with a strip chart recorder or computer point to provide trend

information and the procedure did not direct stationing a dedicated operator to

monitor the pressure instruments. The inspectors concluded that absent a

dedicated operator to observe the pressure indicator, no trend information would

be available to the control room operators to determine whether the described

pressure response had occurred.

Step 1.b of the procedure directed operators to determine whether or not the

instrument air header pressure was stable or rising. The inspectors concluded

this determination would be complicated by the lack of any available trend

information for all of the air header pressure instruments.

Step 2.a of the procedure directed operators to trip the reactors and turbines of

both units in the event of a loss of both instrument air header pressure and

nitrogen header pressure as indicated by the control room instruments. The

inspectors noted the control room instruments only provided pressure indication

for the common headers; there were no available indications for the pressure in

the individual headers of each unit. The inspectors noted that in the event the

backup nitrogen system excess flow check valves either spuriously shut or failed

to open on a complete loss of instrument air, the nitrogen header pressure

instrument would continue to indicate sufficient pressure despite the complete

depressurization of the instrument air headers in both units. In this case,

Step 2.a would direct operators to the Subsequent Actions section of the

procedure to monitor plant response instead of the more appropriate action of

Step 2.b to immediately trip both units.

The inspectors determined the above issues could result in a delay of necessary

operator response actions to mitigate the consequences of an initiating event.

The safety significance and enforcement aspects of this finding are described in

Sections 3.5 and 4.5, respectively.

2.6

Simulator Incorrectly Modeled Plant Response to Loss of Instrument Air

A self-revealing, Green noncited violation of 10 CFR Part 55.46(c)(1) was identified

involving the licensees failure to incorporate a design change in modeling plant

response for the plant-referenced simulator. Specifically, during operator training in the

plant-referenced simulator, the controlled bleedoff valves for the reactor coolant pumps

were modeled to fail closed on a loss of instrument air, whereas the valves in the plant

remained open during an actual loss of instrument air event on June 20, 2007.

The original model regulator installed on the reactor coolant pump (RCP) controlled

bleed off (CBO) Valve 2HV9218 allowed air to bleed off on a loss of instrument air,

enabling the valve actuator to move shut to its fail-safe position. Though not an

intentional design feature of the regulator, the licensee took credit for this feature to shut

Enclosure

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the RCP CBO valve during a loss of instrument air. As such, the plant-referenced

simulator used for operator training modeled the valve going shut during a loss of

instrument air event.

In February 2004, the licensee replaced the existing valve regulator for the RCP CBO

valve with a new style regulator. The new regulators were used because the original

regulator was obsolete. The vendor modified the new regulators to make them leak

tight, removing the unintentional bleed off characteristic. The licensee evaluated the

change in the new regulators and determined the new regulators to be an equivalent

valve as part of Substitute Equivalency Evaluation (SEE) 020040.

On June 20, 2007, both Units 2 and 3 experienced a loss of instrument air event due to

the failure of a three-inch instrument air line header fitting. During this event, the RCP

CBO containment isolation Valve 2HV9218 failed to go closed as the operators

expected. The control room dispatched an operator at the time of the event to

investigate and determine why the valve did not go closed. The operator noted locally

that the valve was open and that pressure was present on the regulator. The control

room subsequently dispatched another operator to independently second-check the

position of the valves. The second operator also noted that the valve was open and that

pressure was present on the regulator. The operators took no other actions at the time

because closure of this valve could cause loss of CBO flow which would have required

the RCPs to be secured.

The inspectors determined that the licensee failed to update the plant-referenced

simulator following the CBO valve regulator change. As a result, operators were trained

that the RCP CBO valves would shut during a loss of instrument air. However, during

the actual loss of instrument air event on June 20 the CBO valve did not go shut as

expected which caused confusion among the operators responding to the event.

The safety significance and enforcement aspects of this finding are described in

Sections 3.6 and 4.6, respectively.

2.7

Failure to Follow Procedure for an Impaired Annunciator

The inspectors identified a Green noncited violation of Technical Specification 5.5.1.1

involving the failure to meet procedural requirements governing impaired annunciators.

Specifically, after the identification of a failed annunciator, operators did not enter the

annunciator in the failed annunciator log or mark the affected annunciator window with

an annunciator compensatory action flag.

The instrument air system at SONGS utilizes a low pressure nitrogen system as a

backup pressure source. An instrument air system pressure drop will automatically

actuate a control valve in the nitrogen system to supplement the instrument air from

liquid nitrogen storage tanks. A flow switch downstream of the control valve is designed

to provide an annunciator in the control when the nitrogen system is actuated. This

annunciator is used as a diagnostic aid and to determine operator actions in

Procedure SO23-13-5, Loss of Instrument Air, Revision 5.

On June 20, 2007, an instrument air header rupture occurred in Unit 2. The inspectors

noted that although the low pressure nitrogen system provided nitrogen to the Unit 3 air

header as designed, the control room annunciator for nitrogen system actuation did not

Enclosure

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alarm. The licensee initiated AR 070601250 on June 29, 2007 to address the failed

annunciator. On July 2, the inspectors noted the failed annunciator was not included in

the impaired annunciator log. The licensee polled two shift managers and determined

that one believed the annunciator should be treated as impaired and requiring

compensatory actions per Procedure SO23-6-29, Operation of Annunciators and

Indicators, Revision 15, and the other shift manager did not. The inspectors concluded

the operators were not consistently implementing the portion of the procedure

concerning impaired annunciators. The licensee subsequently entered the annunciator

in the impaired annunciator log and took the actions specified by Procedure SO23-6-29

for an impaired annunciator.

The safety significance and enforcement aspects of this finding are described in

Sections 3.7 and 4.7, respectively.

2.8

Inadequate Implementation of Corrective Actions for Air Operated Valve Regulators

A Green self-revealing finding was identified associated with the failure of the reactor

coolant pump controlled bleed off valve to shut during a loss of instrument air event.

The licensee failed to adequately implement corrective actions from previously

evaluated industry operating experience for new valve regulators that were installed in

the unit.

In July 2002, industry Operating Experience (OE) was issued which identified potentially

undesirable consequences due a design change to air operated valve regulators that

improved leakage characteristics of the regulators. The old model regulators allowed air

pressure to bleed off on a loss of instrument air, which enabled the valve actuator to

move to its fail-safe position. This was not an intentional design feature of the regulator.

The new regulators were changed to correct this unintentional bleed off and make them

leak tight. The OE was issued to alert users to this change so that if a user had taken

credit for this unintentional bleed off they would be aware of this change and

appropriately address it.

The licensee evaluated this OE and determined that it was applicable to the station.

AR 031001558 was initiated in October 2003 to provide appropriate actions to address

any issues. The licensee identified that this change would not affect air operated valves

that have an associated positioner or controller, or valves that are configured with a

solenoid valve installed between the air regulator and actuator that receives a signal to

vent. Valves without an associated positioner, controller, solenoid valve, or other

configuration to allow for air bleed off could be affected by use of the new regulator.

During this evaluation the licensee also determined that there were not any of the new

regulators in use at the facility at the time.

The licensee had already performed Substitute Equivalency Evaluations (SEE) for

replacing some of the old style regulators with the new style. Based on the results of

the OE review the licensee determined that there was a need to revise the existing

SEEs to require design engineering and procurement engineering to perform a design

change impact review to evaluate the installation configuration. The purpose of this

review was to evaluate whether a design change would be necessary prior to installation

of the new style regulators.

Enclosure

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In February 2004 the licensee replaced the old style regulator with a new style regulator

on the reactor coolant pump (RCP) controlled bleed off (CBO) Valve 2HV9218. This

was evaluated under SEE 020040.

On June 20, 2007 both Units 2 and 3 experienced a loss of instrument air event due to

the failure of a three-inch instrument air line header fitting. During this event, the RCP

CBO containment isolation valve, 2HV9218, failed to go closed as expected. The

licensee dispatched an operator at the time of the event to investigate and determine

why the valve did not go closed. The operator noted that the valve was open and that

pressure was present on the regulator. The licensee took no other actions at the time

because closure of this valve could cause loss of CBO flow which would have required

the RCPs to be secured.

The licensee performed a review of this issue as documented in AR 070600873. During

this review, the licensee determined that the valve should have shut during the loss of

instrument air event and did not because of the new style regulator that had been

installed. The licensee also identified that the SEE appropriately identified the

requirement for design engineering and procurement engineering to perform a design

change impact to evaluate the installation configuration. However, the action by

procurement engineering to require a design change review prior to installation of the

regulator failed due to a known computer software limitation, and the maintenance

engineering review inappropriately determined that there were no applications where the

old regulators did not have a solenoid or bleed off device between the regulator and

solenoid. The licensee also identified that during both of these assessments, the

engineers did not review the UFSAR or any other licensing commitments that credited

bleed down characteristics of the old regulators during a loss of instrument air.

The licensee also performed an extent of condition review to determine if there were any

other instances of these new style regulators being installed in the plant. This review

identified 37 instances of the new regulators being installed in the plant without

performance of a design change impact review.

The safety significance and enforcement aspects of this finding are described in

Sections 3.8 and 4.8, respectively.

3.0

ASSESSMENT

3.1

Ineffective Corrective Actions for Instrument Air Header Ruptures

The failure to take effective corrective actions in response to site and industry operating

experience resulting in a subsequent instrument air header failure was a performance

deficiency. This finding was more than minor since it was associated with the

equipment reliability attribute of the initiating events cornerstone and affected the

cornerstone objective to limit the likelihood of events that upset plant stability and

challenge critical safety functions. This finding required a Phase 2 analysis per the

Manual Chapter 0609, Significance Determination Process, Phase 1 Worksheets since

the loss of instrument air is a transient initiator resulting in the loss of the feedwater

system which is part of the power conversion system which can be used to mitigate the

consequences of an accident. The inspectors performed a Phase 2 analysis using

Appendix A, Technical Basis for At-Power Significance Determination Process, and the

Phase 2 worksheets for SONGS. The inspectors assumed that the exposure period

Enclosure

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was greater than 30 days, that the performance deficiency increased the likelihood that

a complete loss of instrument air would occur, and that there was no affect on mitigating

systems other than those modeled in the risk-informed notebook. Details of the

Phase 2 analysis and a subsequent Phase 3 analysis are documented in Attachment 3.

Based on the results of the Phase 3 analysis, the finding was determined to be of very

low safety significance (Green) because of the availability of the diverse auxiliary

feedwater system and the ability of the operators to depressurize the steam generators

and utilize the condensate system for heat removal. These results were evaluated by a

senior reactor analyst. In addition, the senior reactor analyst determined the impact of

this performance deficiency on the likelihood of the large-early release frequency.

These evaluations indicated that the impacts were also of very low safety significance.

This finding has a crosscutting aspect in the area of problem identification and

resolution associated with operating experience in that the licensee failed to effectively

implement changes to station processes, procedures, and equipment in response to

operating experience involving improperly made instrument air system joints P.2(b).

3.2

Failure to Follow Abnormal Operating Instruction for the Loss of Instrument Air

The failure to follow station procedures to monitor nitrogen tank levels and oxygen

concentrations in enclosed rooms where operator actions may have been required was

a performance deficiency. This finding was more than minor since it was associated

with the human performance attribute of the initiating events cornerstone and affected

the cornerstone objective to limit the likelihood of events that upset plant stability and

challenge critical safety functions. This finding required a Phase 2 analysis in

accordance with the Manual Chapter 0609, Significance Determination Process,

Phase 1 Worksheets since the loss of instrument air is a transient initiator resulting in

the loss of the feedwater system which is part of the power conversion system which

can be used to mitigate the consequences of an accident. The inspectors performed a

Phase 2 analysis using Appendix A, Technical Basis for At-Power Significance

Determination Process, and the Phase 2 worksheets for SONGS. The inspectors

assumed that the exposure period was greater than 30 days, that the performance

deficiency increased the likelihood that a complete loss of instrument air would occur,

and that there was no affect on mitigating systems other than those modeled in the risk-

informed notebook. Based on the results of the Phase 2 analysis, the finding was

determined to be of very low safety significance because of the low likelihood of a

complete loss of instrument air and the availability of the auxiliary feedwater system.

These results were evaluated by a senior reactor analyst. In addition, the senior reactor

analyst determined the impact of this performance deficiency on the risk of external

events and on the likelihood of the large-early release frequency. These evaluations

indicated that the impacts were also of very low safety significance.

The cause of this finding has a crosscutting aspect in the area of human performance

associated with resources because licensee personnel were not adequately trained on

the operation of the low pressure nitrogen system to effectively implement the abnormal

operating instruction H.2(b).

Enclosure

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3.3

Inadequate Evaluation Results in Runout of Component Cooling Water Pump

The failure to adequately evaluate the total system hydraulic effects prior to

implementing a design change to supply nitrogen to the NCL isolation valves was a

performance deficiency. This finding was greater than minor because it was associated

with the mitigating systems cornerstone attribute of design control and affected the

associated cornerstone objective to ensure the availability, reliability, and capability of

systems that respond to initiating events to prevent undesirable consequences. The

finding did not affect the initiating events cornerstone functions of the component

cooling water system because the condition would only have existed given a loss of

instrument air initiator had already occurred. In accordance with NRC Inspection

Manual Chapter 0609, Appendix A, Phase 1 Worksheet, Significance Determination

Process (SDP) Phase 1 Screening Worksheet for the Initiating Events, Mitigating

Systems, and Barriers Cornerstones, this finding was determined to be of very low

safety significance because the finding was a design deficiency confirmed not to result

in a loss of operability per Part 9900, Technical Guidance, Operability Determination

Process for Operability and Functional Assessment.

3.4

Ineffective Corrective Actions for a Failed Control Room Annunciator

The failure to perform adequate corrective actions for a failed control room annunciator

resulting in the failure of the annunciator to function during an actual event was a

performance deficiency. This finding was more than minor since it was associated with

the human performance attribute of the initiating events cornerstone and affected the

cornerstone objective to limit the likelihood of events that upset plant stability and

challenge critical safety functions. This finding required a Phase 2 analysis in

accordance with the Manual Chapter 0609, Significance Determination Process,

Phase 1 Worksheets since the loss of instrument air is a transient initiator resulting in

the loss of the feedwater system which is part of the power conversion system which

can be used to mitigate the consequences of an accident. The inspectors performed a

Phase 2 analysis using Appendix A, Technical Basis for At-Power Significance

Determination Process, and the Phase 2 worksheets for SONGS. The inspectors

assumed that the exposure period was greater than 30 days, that the performance

deficiency increased the likelihood that a complete loss of instrument air would occur,

and that there was no affect on mitigating systems other than those modeled in the risk-

informed notebook. Based on the results of the Phase 2 analysis, the finding was

determined to be of very low safety significance because of the low likelihood of a

complete loss of instrument air and the availability of the auxiliary feedwater system.

These results were evaluated by a senior reactor analyst. In addition, the senior reactor

analyst determined the impact of this performance deficiency on the risk of external

events and on the likelihood of the large-early release frequency. These evaluations

indicated that the impacts were also of very low safety significance.

This finding has a crosscutting aspect in the area of problem identification and

resolution associated with the corrective action program in that the licensee failed to

thoroughly evaluate the failed annunciator such that the resolution appropriately

addressed the causes P.2(c).

Enclosure

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3.5

Inadequate Procedure for a Loss of Instrument Air

The failure to provide adequate procedural guidance to immediately diagnose and

properly respond to an initiating event was a performance deficiency. This finding was

more than minor because it was associated with the procedure quality attribute of the

mitigating systems cornerstone and affected the cornerstone objective to ensure the

availability, reliability and capability of systems that respond to initiating events, in that a

less than adequate abnormal operating procedure could have prevented operators from

promptly tripping the reactor, allowing conditions to continue to degrade and resulting in

a demand on the reactor protection system. Using the Significance Determination

Process Phase 1 Screening Worksheet in Appendix A of Inspection Manual Chapter 0609, the inspectors determined this finding had very low safety significance because it

did not result in an actual loss of safety function per Part 9900, Technical Guidance,

Operability Determination Process for Operability and Functional Assessment.

This finding has a crosscutting aspect in the area of human performance associated

with resources in that the licensee failed to provide operators with complete, accurate,

and up-to-date procedures H.2(c).

3.6

Simulator Incorrectly Modeled Plant Response to Loss of Instrument Air

The failure to ensure that the plant-referenced simulator correctly replicated expected

plant response to transient conditions was a performance deficiency. This finding was

greater than minor because it was associated with the mitigating systems cornerstone

attribute of human performance and affected the associated cornerstone objective to

ensure the availability, reliability, and capability of systems that respond to initiating

events to prevent undesirable consequences. The inspectors evaluated this finding

using the Appendix I, Licensed Operator Requalification Significance Determination

Process worksheets of Manual Chapter 0609 because the finding is a requalification

training issue related to simulator fidelity. Block 12 of the Appendix I flow chart requires

the inspector to determine if deviations between the plant and simulator could result in

negative training or could have a negative impact on operator actions. Negative

Training is defined, in a later version of the standard (ANSI 3.5-1998), as training on a

simulator whose configuration or performance leads the operator to incorrect response

or understanding of the reference unit. The licensee has committed to this version of

the ANS/ANSI standard for its simulator testing program for the plant-referenced

simulator. During the event of June 20, 2007, operators were influenced by negative

training on the simulator to question control room indications and locally independently

verify valve positions because valves in the plant failed to respond to a loss of

instrument air as modeled in the simulator. Therefore, differences between the simulator

and plant did have a negative impact on operator actions. The finding is of very low

safety significance because the discrepancy did not have an adverse impact on operator

actions such that safety related equipment was made inoperable during normal

operations or in response to a plant transient.

This finding has a crosscutting aspect in the area of human performance associated

with resources in that the licensee did not provide operators with adequate facilities and

equipment for use in operator training H.2(d).

Enclosure

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3.7

Failure to Follow Procedure for an Impaired Annunciator

The failure to follow station procedures resulting in an untracked nonfunctional

annunciator was a performance deficiency. This finding was more than minor since it

was associated with the human performance attribute of the initiating events

cornerstone and affected the cornerstone objective to limit the likelihood of events that

upset plant stability and challenge critical safety functions. This finding required a

Phase 2 analysis in accordance with the Manual Chapter 0609, Significance

Determination Process, Phase 1 Worksheets since the loss of instrument air is a

transient initiator resulting in the loss of the feedwater system which is part of the power

conversion system which can be used to mitigate the consequences of an accident.

The inspectors performed a Phase 2 analysis using Appendix A, Technical Basis for

At-Power Significance Determination Process, and the Phase 2 worksheets for

SONGS. The inspectors assumed that the exposure period was greater than 30 days,

that the performance deficiency increased the likelihood that a complete loss of

instrument air would occur, and that there was no affect on mitigating systems other

than those modeled in the risk-informed notebook. Based on the results of the Phase 2

analysis, the finding was determined to be of very low safety significance because of the

low likelihood of a complete loss of instrument air and the availability of the auxiliary

feedwater system. These results were evaluated by a senior reactor analyst. In

addition, the senior reactor analyst determined the impact of this performance deficiency

on the risk of external events and on the likelihood of the large-early release frequency.

These evaluations indicated that the impacts were also of very low safety significance.

This finding has a crosscutting aspect in the area of human performance associated

with resources because the operators were not sufficiently trained to consistently

implement the annunciator operating procedure H.2(b).

3.8

Inadequate Implementation of Corrective Actions for Air Operated Valve Regulators

The failure to adequately implement corrective actions from industry OE to perform a

design change impact review was a performance deficiency. The finding was greater

than minor because it was associated with the mitigating systems cornerstone attribute

of design control and affected the associated cornerstone objective to ensure the

availability, reliability, and capability of systems that respond to initiating events to

prevent undesirable consequences. Using Manual Chapter 0609, Significance

Determination Process, Phase 1 Worksheet, the finding is determined to have very low

safety significance because the condition only affected the mitigation systems

cornerstone and it was confirmed not to result in loss of operability per Part 9900,

Technical guidance, Operability Determination Process for Operability and Functionality

Assessment.

4.0

ENFORCEMENT

4.1

Ineffective Corrective Actions for Instrument Air Header Ruptures

No violation of regulatory requirements occurred since the affected equipment was not

safety-related. This finding was entered into the licensees corrective action program as

Action Request AR 070600867 and is identified as FIN 05000361;362/2007013-01,

Ineffective Corrective Actions for Instrument Air Header Ruptures.

Enclosure

-30-

4.2

Failure to Follow Abnormal Operating Instruction for the Loss of Instrument Air

Technical Specification 5.5.1.1 requires written procedures to be implemented as

recommended by Regulatory Guide 1.33, Revision 2, Appendix A, February 1978.

Section 6.b of Appendix A recommends procedures governing actions to be taken on a

loss of instrument air. Step 3.h of Procedure SO23-13-5, Loss of Instrument Air,

Revision 5, required notification of all building operators of the possibility of oxygen

deficient areas, monitoring of enclosed spaces for oxygen levels prior to entry, and

monitoring of liquid nitrogen inventory following actuation of the backup nitrogen system

following an instrument air leak. Contrary to this requirement, operators failed to

implement these actions following actuation of the nitrogen system due to an instrument

air line break on June 20, 2007. Because this violation was of very low safety

significance and was entered in the corrective action program as Action Request

AR 070700291, this violation is being treated as an NCV consistent with Section VI.A.1

of the NRC Enforcement Policy: NCV 05000361;362/2007013-02, Failure to Follow

Abnormal Operating Instruction for the Loss of Instrument Air.

4.3

Inadequate Evaluation Results in Runout of Component Cooling Water Pump

10 CFR Part 50, Appendix B, Criterion III, Design Control, requires, in part, that

measures be established to assure that applicable regulatory requirements and the

design basis, as specified in the license application, are correctly translated into

specifications, drawings, procedures, and instructions. It further states that design

control measures shall provide for verifying or checking the adequacy of design, such as

by the performance of design reviews, by the use of alternate or simplified calculational

methods, or by the performance of a suitable testing program. Contrary to the above,

the licensee failed to verify the adequacy of the design associated with the modification

of the CCW NCL isolation valves installed in 1995. Because this finding is of very low

safety significance and has been entered into the corrective action program as Action

Requests AR 070700051 and 070600872, this violation is being treated as an NCV

consistent with Section VI.A of the NRC Enforcement Policy:

NCV 05000361;362/2007013-03, Inadequate Evaluation Results in Runout of

Component Cooling Water Pump.

4.4

Ineffective Corrective Actions for a Failed Control Room Annunciator

No violations of NRC requirements were identified during the review of this issue

because instrument air is not a safety related system. The licensee entered this issue

into the corrective action program as Action Request AR 070601250:

FIN 05000361;362/2007013-04, Ineffective Corrective Actions for a Failed Control

Room Annunciator.

4.5

Inadequate Procedure for a Loss of Instrument Air

Technical Specification 5.5.1.1 requires written procedures to be implemented as

recommended by Regulatory Guide 1.33, Quality Assurance Program Requirements,

Revision 2, Appendix A, February 1978. Section 6.b of Appendix A of Regulatory Guide 1.33 recommends procedures governing actions to be taken on a loss of instrument air.

American National Standard ANS-3.2, Administrative Controls and Quality Assurance

for the Operational Phase of Nuclear Power Plants, February 1976, describes the

requirements for the quality of the procedures specified in Regulatory Guide 1.33.

Enclosure

-31-

Section 5.3.9.1(4) of Standard ANS-3.2 requires emergency procedures to specify

immediate actions for operation of controls or confirmation of automatic actions that are

required to stop the degradation of conditions and mitigate consequences. Contrary to

this requirement, since its release on May 4, 2006, Revision 5 of Procedure SO23-13-5,

Loss of Instrument Air, did not provide adequate guidance for operators to immediately

diagnose and properly respond to a complete loss of the instrument air system.

Because this violation was of very low safety significance and was entered in the

corrective action program as Action Request AR 070801151, this violation is being

treated as an NCV consistent with Section VI.A.1 of the NRC Enforcement Policy:

NCV 05000361;362/2007013-05, Inadequate Procedure for Loss of Instrument Air.

4.6

Simulator Incorrectly Modeled Plant Response to Loss of Instrument Air

10 CFR Part 55.46(c)(1) requires, in part, that the plant-referenced simulator must

demonstrate expected plant response to transient conditions. Contrary to this

requirement, the response modeled by the licensees simulator for the reactor coolant

pump controlled bleedoff valves did not demonstrate expected plant response to the

June 20, 2007 loss of instrument air event. Because this violation was of very low safety

significance and was entered in the corrective action program as Action Requests

AR 070600873 and 070900160, this violation is being treated as an NCV consistent with

Section VI.A.1 of the NRC Enforcement Policy: NCV 05000361;362/2007013-06,

Simulator Incorrectly Modeled Plant Response to Loss of Instrument Air.

4.7

Failure to Follow Procedure for an Impaired Annunciator

Technical Specification 5.5.1.1 requires written procedures to be implemented as

recommended by Regulatory Guide 1.33, Revision 2, Appendix A, February 1978.

Section 1.c of Appendix A recommends administrative procedures governing equipment

control. Section 6.2.2 of Procedure SO23-6-29, Operation of Annunciators and

Indicators, Revision 15, required tracking of impaired annunciators requiring

compensatory actions. Contrary to this requirement, operators failed to track an

impaired annunciator from June 29 to July 2, 2007. Because this violation was of very

low safety significance and was entered in the corrective action program as Action

Request AR 070700291, this violation is being treated as an NCV consistent with

Section VI.A.1 of the NRC Enforcement Policy: NCV 05000361;362/2007013-07,

Failure to Follow Procedure for an Impaired Annunciator.

4.8

Inadequate Implementation of Corrective Actions for Air Operated Valve Regulators

No violation of regulatory requirements occurred. This finding was entered in the

licensees corrective action program as Action Request AR 070600873:

FIN 05000361;362/2007013-07, Inadequate Implementation of Corrective Actions for

Air Operated Valve Regulators.

Enclosure

-32-

4OA6 Meetings, Including Exit

On July 2, 2007, and September 13, 2007, the results of this inspection were presented

to Dr. R. Waldo, Vice President Nuclear Generation, and other members of his staff who

acknowledged the findings. Additionally on October 11, 2007, the final results of this

inspection were presented to A. Scherer, Manager, Nuclear Regulatory Affairs, and

other members of his staff who acknowledged the findings. The inspector confirmed

that no proprietary material was examined during the inspection.

ATTACHMENT 1: SUPPLEMENTAL INFORMATION

ATTACHMENT 2: SPECIAL INSPECTION CHARTER

ATTACHMENT 3: SIGNIFICANCE DETERMINATION EVALUATION

Attachment 1

A1-1

SUPPLEMENTAL INFORMATION

KEY POINTS OF CONTACT

Licensee Personnel

K. Flynn, Site Operating Experience Coordinator

S. Gardner, Engineer, Nuclear Regulatory Affairs

B. Katz, Vice President, Nuclear Oversight and Regulatory Affairs

L. Kelly, Engineer, Nuclear Regulatory Affairs

M. Love, Manager, Maintenance

M. Mostafa, Consulting Engineer

K. Rauch, Operations Training Manager

A. Scherer, Manager, Nuclear Regulatory Affairs

P. Schofield, System Maintenance Engineer Supervisor

J. Summy, System Engineering Manager

D. Tuttle, Systems Engineer

T. Vogt, Manager, Operations

R. Waldo, Vice President, Nuclear Generation

D. Wilcockson, Manager, Plant Operations

C. Williams, Manager, Compliance

LIST OF ITEMS OPENED, CLOSED, AND DISCUSSED

Opened and Closed

05000361;

362/2007013-01

FIN

Ineffective Corrective Actions for Instrument Air Header

Ruptures

05000361;

362/2007013-02

NCV

Failure to Follow Abnormal Operating Instruction for the

Loss of Instrument Air

05000361;

362/2007013-03

NCV

Inadequate Evaluation Results in Runout of Component

Cooling Water Pump

05000361;

362/2007013-04

FIN

Ineffective Corrective Actions for a Failed Control Room

Annunciator

05000361;

362/2007013-05

NCV

Inadequate Procedure for a Loss of Instrument Air

05000361;

362/2007013-06

NCV

Simulator Incorrectly Modeled Plant Response to a Loss of

Instrument Air

05000361;

362/2007013-07

NCV

Failure to Follow Procedure for an Impaired Annunciator

05000361;

362/2007013-08

FIN

Inadequate Implementation of Corrective Actions for Air

Operated Valve Regulators

Attachment 1

A1-2

LIST OF DOCUMENTS REVIEWED

Procedures

Number

Title

Revision

SO23-6-29

Operation of Annunciators and Indicators

15

SO23-13-5

Loss of Instrument Air

5

SO123-0-A8

Trip/Transient and Event Review

1

SO23-12-1

Standard Post Trip Actions

21

SO23-12-2

Reactor Trip Recovery

18

SO23-1-1

Instrument Air System Operation

17

SO123-XV-5.3

Maintenance Rule Program

9

SO23-6-29

Operation of Annunciators and Indicators

15

SO123-XV-50.39.1

Division Investigative Reports

0

SO123-I-1.42

Maintenance Division Experience Report

0

SO123-XV-50

Corrective Action Process

6

Action Requests

070400754

060101956

070400766

070600867

051000080

050600477

070600877

050901305

041101801

060101956

050901037

070600914

070600867

070600872

960500111

031001558

041000977

010601495

070600873

041002146

061001297

070600914

040901643

060101956

070500196

070600870

070601250

070501276

070400776

060200898

Work Orders/Maintenance Work Orders

07061161000

06012099000

94062628000

94062628001

07041277000

07061216000

Attachment 1

A1-3

07041921000

06020520000

05111108000

05111009000

05061587000

05061588000

06020580000

05111105000

05111106000

05111107000

07051780000

05061583000

05061589000

05061590000

06021071000

07050347000

05061584000

05061585000

05061586000

07061216000

07061324000

07061325000

Drawings

Number

Title

Revision

F-10946M

Component Cooling Water System No. 1203

21

F-10543M

Component Cooling Water System No. 1203

15

40191A

Compressed Air System

15

40191B

Compressed Air System

21

40191C

Compressed Air System

19

40191D

Compressed Air System

34

40191DSO3

Compressed Air System

19

40191F

Compressed Air System

13

40191X

Compressed Air System

2

40190C

Respiratory Service Air

22

40192A

Auxiliary Gas System

20

40192B

Auxiliary Gas System

16

40191GSO3

Instrument Air Distribution

7

40191E-10

Instrument Air System

10

40191G

Instrument Air Distribution

8

Calculations

M-DSC-429, Evaluation of Joint Restraint Clamp on Instrument Air Piping, Revision 0

M-0091, Backup Nitrogen for the Instrument Air System Equipment Sizing, Revision 0

IPE-HC-006, Operator Action Summary Data Sheet Post-Initiator Human Error Probability

Calculation Worksheet

Attachment 1

A1-4

Miscellaneous Information

PRA-07-007, PRA Preliminary Evaluation of Loss of Instrument Air Event Resulting in Unit 2

Trip, Dated June 22, 2007

Operator Action Summary Data Sheet Post-Initiator Human Error Probability Calculation

Worksheet

DBD-SO23-540, Instrument Air/Dedicated Backup Nitrogen System, Revision 6

Engineering Change Package 070600914-6, Revision 0

SONGS 2 Instrument Air System Failed Fitting Metallurgical Evaluation

SONGS System Health Reports for the Instrument Air System and Vendor Owned Nitrogen

Package

Failure Analysis Report No.94-006, Failure Analysis of the Instrument Air Fitting for

Temperature Gauge 2/3TI5380

Failure Analysis Report No.94-009, Failure Analysis of the Instrument Air Fitting for

Temperature Gauge 2/3TI5380, Supplement 1, Dated October 3, 1994

DBD-SO23-540, Instrument Air/Dedicated Backup Nitrogen Systems, Revision 6

Maintenance Rule Guide Book, Dated February 2004

SD-SO23-400, Component Cooling Water System, Revision 6

Meeting Agenda Maintenance Rule Expert Panel, Dated June 21, 2007

Regulatory Guide 1.160, Monitoring the Effectiveness of Maintenance at Nuclear Power Plants,

Revision 2

Licensee Event Report No. 2007-001-01, Revision 1, Dated August 24, 2004

Substitute Equivalency Evaluation 020040, Substitute 67CFR-237 Series Regulator for 67AFR-

237, Revision 1

A2-1

Attachment 2

June 26, 2007

MEMORANDUM TO: Geoffrey Miller, Senior Resident Inspector, Grand Gulf

Jeffrey Josey, Resident Inspector, Arkansas Nuclear One

FROM:

Arthur T. Howell III, Director, Division of Reactor Projects /RA AVegel for/

SUBJECT:

SPECIAL INSPECTION CHARTER TO EVALUATE THE SAN ONOFRE

NUCLEAR GENERATING STATION INSTRUMENT AIR FAILURE

A Special Inspection Team is being chartered in response to the Unit 2 San Onofre Nuclear

Generating Station loss of instrument air event on June 20, 2007. You are hereby designated

as the Special Inspection Team members. Mr. Miller is designated as the team leader. The

assigned SRA to support the team is David Loveless.

A.

Basis

On June 20, 2007, a 3-inch diameter instrument air line failed. At SONGS, instrument

air is a shared system, but the system is equipped with certain protective features

(excess flow check valves) to ensure that a failure in the piping system on one unit does

not significantly affect instrument air pressure on the other unit. On Unit 2, instrument

air pressure dropped significantly, from approximately 110 psig to about 43 psig. The

loss of instrument air pressure caused the feedwater control valves to stop functioning

and water level in the steam generators increased in an uncontrolled manner.

Operators manually tripped the reactor. The operators also lost control of the steam

dumps to the condenser (the normal heat removal method) and controlled steam

generator pressure and decay heat removal using the steam generator atmospheric

dump valves. The chemical and volume control system letdown function auto-isolated

and operators manually controlled pressurizer level with a charging pump. On Unit 3,

the pressure drop was not as significant but appeared to be more than expected.

However, Unit 3 Operators maintained control of all functions during the event.

Operators were able to isolate the failed instrument air line approximately 30 minutes

later and regained control of the Unit 2 condenser steam dumps.

During post-trip discussions with the operators, one operator stated that they had

experienced other instrument air piping failures but the affected piping was much

smaller and did not significantly challenge plant operations. One such failure occurred

in 1994.

This Special Inspection Team is chartered to review the circumstances related to

historical and present instrument air piping problems and assess the effectiveness of the

A2-2

Attachment 2

licensees actions for resolving these problems. The team will also assess the

effectiveness of the immediate actions taken by the licensee in response to the loss of

instrument air event on June 20, 2007.

B.

Scope

The team is expected to address the following:

1.

Develop a chronology (time-line) that includes significant event elements.

2.

Evaluate the operator response to the event. Ensure that operators responded

in accordance with plant procedures and took appropriate mitigating actions.

3.

Develop an understanding of the interface between instrument air and other risk

important systems, including the possible reliance, either short term or long term,

of safety related components on instrument air.

4.

Evaluate the plant response to the event. Ensure that all systems responded as

designed. In particular, verify that design provisions, intended to prevent failure

in one units piping from causing an excessive pressure drop in the other unit,

worked properly (see UFSAR Sections 9.3.1.1.E and 9.3.1.2.3).

5.

Assess the licensees root cause determination for the instrument air piping

failure, the extent of condition review, the common cause evaluation and

corrective measures. Evaluate whether the timeliness of the corrective

measures are consistent with the safety significance of the problems.

6.

Identify previous instrument air piping problems that may have been precursors

to the June 20 event, including one event in 1994. Evaluate the licensees

corrective measures and extent of condition reviews for those problems.

7.

Evaluate the licensees instrument air system maintenance and testing

programs. Verify that the programs are adequate and that the licensee is

following the program provisions. Pay particular attention to the historical health

of the instrument air compressors and piping system.

8.

Evaluate pertinent industry operating experience that represent potential

precursors to the June 20 event, including the effectiveness of licensee actions

taken in response to the operating experience. As a minimum include Generic Letter 88-14, Instrument Air Supply System Problems Affecting Safety-Related

Equipment, including the licensees response to the generic letter; and NRC

Information Notice 2002-29,Recent Design Problems in Safety Functions of

Pneumatic Systems. You may also use NUREG 1837, Regulatory

Effectiveness Assessment of Generic Issue 43 and Generic Letter 88-14, to aid

in your assessment. The NUREG can be found at:

http://www.nrc.gov/reading-rm/doc-collections/nuregs/staff/sr1837/sr1837.pdf

A2-3

Attachment 2

9.

Determine if there are any potential generic issues related to the failure of the

SONGS instrument air piping. Promptly communicate any potential generic

issues to Region IV management.

10.

Collect data as necessary to support a risk analysis. Work closely with the

Senior Reactor Analyst during this inspection.

C.

Guidance

Inspection Procedure 93812, Special Inspection, provides additional guidance to be

used by the Special Inspection Team. Your duties will be as described in Inspection

Procedure 93812. The inspection should emphasize fact-finding in its review of the

circumstances surrounding the event. It is not the responsibility of the team to examine

the regulatory process. Safety concerns identified that are not directly related to the

event should be reported to the Region IV office for appropriate action.

The Team will report to the site, conduct an entrance, and begin inspection no later than

June 27, 2007. While on site, you will provide daily status briefings to Region IV

management, who will coordinate with the Office of Nuclear Reactor Regulation, to

ensure that all other parties are kept informed. A report documenting the results of the

inspection should be issued within 30 days of the completion of the inspection.

This Charter may be modified should the team develop significant new information that

warrants review. Should you have any questions concerning this Charter, contact me at

(817) 860-8147.

A3-1

Attachment 3

ATTACHMENT 3

SIGNIFICANCE DETERMINATION EVALUATION

San Onofre Nuclear Generating Station

Failure of Instrument Air System Header

Phase 3 Analysis

A.

Brief Description of Issue

On June 20, 2007, instrument air pressure at San Onofre Unit 2 dropped significantly

following the separation of a 3-inch fitting in the system air header located in the

auxiliary building. This caused the feedwater control valves to stop functioning, resulting

in an uncontrolled increase in steam generator water level. Operators manually tripped

the Unit 2 reactor. The loss of instrument air caused containment isolations and a loss

of most power conversion system functions.

The licensee performed a metallurgical analysis of the failed joint and determined that

the cause of the failure was poor workmanship during initial installation. The analysis

concluded that the joint was most likely leaking since initial plant startup because, during

original installation the brazing activity resulted in inadequate solder coverage and the

connection had continued to deteriorate throughout the life of the plant. During a

walkdown of the system in both units, licensee personnel discovered that 32 other large

fittings were leaking at the joint.

A special inspection team reviewed the licensees root cause evaluation and

metallurgical evaluation for this event. During their review, the team noted that there

had been a previous similar air header failure at San Onofre in June 1994. At that time,

both Units 2 and 3 experienced a loss of instrument air following the failure of an

improperly soldered joint. A metallurgical analysis conducted in 1994 concluded that

this joint had also likely been leaking since initial startup from inadequate solder

coverage.

A large amount of industry operating experience has been available that deals with

soldered joint issues. During the original evaluation of related operational experience

reports, done by the licensee in 1992, they failed to properly assess the impact to San

Onofre. Engineers had determined that if failures were going to have occurred because

of inadequate fit-up and/or solder penetration, the failures would have occurred within a

relatively short time frame. Therefore, they assumed that related industry experience

was not applicable to San Onofre. The team also determined that the licensee failed to

adequately reassess their position when they experienced an air line joint failure in

1994, and as a result, failed to take effective corrective actions following that failure.

B.

Statement of the Performance Deficiency

The licensee failed to take effective corrective actions in response to the failure of an

improperly made soldered joint in the instrument air header affecting both units at San

A3-2

Attachment 3

Onofre in June 1994. Specifically, contrary to Section 6.2.3 of

Procedure SO-123-I-1.42, Maintenance Division Experience Report, Revision 0, the

licensee failed to implement corrective actions to prevent recurrence for an equipment

failure with the potential to cause a significant plant transient, and failed to appropriately

consider previous industry and plant experience similar to the event. Additionally,

licensee personnel failed to properly evaluate and take corrective actions based on

industry operating experience through 2006 involving improperly made soldered joints in

instrument air systems. As a result, an additional failure of an improperly made

instrument air header joint occurred at San Onofre on June 20, 2007, resulting in a

complete loss of instrument air to Unit 2.

C.

Significance Determination Basis

1.

Phase 1 screening logic, results and assumptions

In accordance with NRC Inspection Manual Chapter 0612, Appendix B, "Issue

Screening," the team determined that this finding represented a licensee

performance deficiency. The team then determined that the issue was more

than minor because the finding was associated with the equipment performance

attribute and affected the initiating events cornerstone objective to limit the

likelihood of those events that upset plant stability and challenge critical safety

functions during shutdown as well as power operations.

The team evaluated this finding using the, "SDP Phase 1 Screening Worksheet

for the Initiating Events, Mitigating Systems, and Barriers Cornerstones,"

provided in Manual Chapter 0609, Appendix A, "Significance Determination of

Reactor Inspection Findings for At-Power Situations." A Phase 2 estimation was

required because the associated performance deficiency represented an

increase in both the likelihood of a reactor trip and the probability that the power

conversion system would be unavailable.

2.

Phase 2 Risk Estimation

In accordance with Manual Chapter 0609, Appendix A, Attachment 1, User

Guidance for Significance Determination of Reactor Inspection Findings for At-

Power Situations, the team evaluated the subject findings using the Risk-

Informed Inspection Notebook for San Onofre Nuclear Generating Station

(SONGS) Units 2 and 3, Revision 2.1. The dominant affected accident

sequences are provided in Table 1. The team assumed that the exposure period

was greater than 30 days, that the performance deficiency increased the

likelihood that a complete loss of instrument air would occur, and that there was

no affect on mitigating systems other than that modeled in the risk-informed

notebook.

A3-3

Attachment 3

TABLE 1

Increased Likelihood of a Complete Loss of Instrument Air

Phase 2 Sequences

Initiating Event

Sequence

Mitigating Functions

Results

Loss of Instrument

Air

1

LOIA-AFW

7

2

LOIA-RCPTRIP-HPR

9

3

LOIA-RCPTRIP-CNT

9

4

LOIA-RCPTRIP-EIHP

9

Using the counting rule worksheet, the result from this estimation indicated that

this finding was of very low safety significance (GREEN).

A senior reactor analyst reviewed the Phase 2 estimation and determined that

the risk-informed notebook and the licensees PRA had a common error that

significantly underestimated the risk of this deficiency. The loss of instrument air

initiating event frequency had been established as 6.4 x 10-5/year by assuming

that a loss of all active instrument air system components as well as a loss of the

backup nitrogen system was required to realize a complete loss of instrument

air. However, there are many system breaches and other passive component

failures that would prevent the backup nitrogen system from performing its

function.

Therefore, the analyst determined that the finding should be evaluated using the

Phase 3 process.

3.

Phase 3 Analysis

The analyst quantified the change in risk of the subject performance deficiency

as indicated in the paragraphs below. The change in internal event risk was

estimated as 4.7 x 10-7 over an entire assessment period. The risk related to

seismic events changed by 4.1 x 10-7 and that related to internal fires by

9.5 x 10-9. This resulted in a total change in CDF of 8.9 x 10-7. Therefore, the

analyst determined that the subject finding was of very low safety significance

(Green).

Internal Initiating Events:

The following techniques were used in this evaluation.

a.

The analyst quantified the internal risk using the Standardized Plant

Analysis Risk (SPAR) Model for San Onofre 2 & 3, Revision 3.21, created

in October 2005. The analyst modeled a loss of instrument air by

assuming that the affect was equivalent to a transient with a complete

loss of the power conversion system with the possibility of a recovery of

A3-4

Attachment 3

condensate by bypassing the feedwater isolation and depressurizing the

steam generators. The likelihood of a loss of instrument air was then

increased to 6.8 x 10-2/year as a result of the performance deficiency.

The resulting quantification indicated an increase over the baseline core

damage frequency of 4.7 x 10-7 over a 365-day exposure.

b.

The licensee developed a model for analyzing the internal risk associated

with the event using the current version of their PRA model. The licensee

revised the model by setting the loss of instrument air initiating event

frequency to 0.5 indicating that operators could have recovered the

condition prior to a reactor trip. Additionally, the licensee estimated that

50% of the transients initiated by an instrument air system breach would

be recovered by operators prior to core damage. No other initiators were

considered to be applicable to this condition.

Licensee analysts changed their model to show that the controlled

bleedoff valves remained open. As documented in Licensee Event

Report 50-361/2007001, the licensees conditional core damage

probability (CCDP) for this event was 3.3 x 10-6.

At the analysts request, the licensee provided a CCDP for a generic loss

of instrument air. The value provided by their model was 4.85 x 10-6.

The analyst converted the licensees CCDP to a change in the core

damage frequency by multiplying it with the calculated initiating event

frequency. The result was 3.29 x 10-7 over the 1-year assessment

period. This tends to corroborate the analysts value and suggests that

the initiating event frequency is the primary difference between the two

values.

In performing the Phase 3 evaluation, the following influential assumptions were

made by the analyst:

a.

The failure of a large fitting in the instrument air system at the San

Onofre site would cause a reactor trip on the subject unit at least 1/2 the

time. This was based on the 2 historical failures in the units.

b.

This condition existed for many years for both units and should be

evaluated over the most recent 1-year assessment period.

c.

The baseline failure rate of the instrument air system should have been

the boolean combination of the system components including the backup

instrument air system. Given intact system piping, this was calculated by

the licensee to be 6.4 x 10-5/year.

d.

The instrument air system had been functional for 22.09 reactor-years.

This value is the number of years that either or both reactors were critical.

Such an assumption was used because the system is common to both

units.

A3-5

Attachment 3

e.

Because the condition causing failures in the instrument air headers was,

in part, an aging issue and because there were 32 additional leaking

fittings identified in the system, the analyst assumed that an additional

failure was eminent prior to repair (eg: 3 failures were assumed to have

occurred).

f.

Upon loss of instrument air, the condensate system is potentially still

available given operators depressurize the reactor coolant system and

manually realign the condensate system to bypass the feedwater

regulating valves.

The following calculations were performed during this analysis:

a.

The analyst calculated the revised likelihood of a loss of instrument air.

The result of 1.36 x 10-1 was calculated based on the 2 historical

breaches of the system, an additional postulated breach to account for

the aging affect, and a service time of 22.09 reactor-years.

b.

As stated above, historically San Onofre has had 2 events that involved

breaches of an instrument air header. On one of these occasions,

operators were able to identify and limit the leak to prevent a reactor

transient. Therefore, the initiating event likelihood was reduced by 50%

to 6.8 x 10-2.

c.

The analyst estimated the nonrecovery probability for the operators

depressurizing the reactor coolant system and feeding the steam

generators using the condensate system. Three components went into

this analysis: 1) the human error probability calculated using the SPAR-H

method; 2) the probability that the atmospheric dump system failed; and

3) the probability that the condensate system failed mechanically. The

last two probabilities were calculated by solving appropriate portions of

the SPAR fault trees. The overall nonrecovery probability was calculated

to be 9.3 x 10-2.

d.

The analyst used the SPAR model to quantify the internal change in risk

for a loss of instrument air by modeling a loss of condensate, bypass

capability, and main feedwater. The analyst set all initiators to the house

event, FALSE, with the exception of transients. The transient initiator

was used as a surrogate initiator for the loss of instrument air, and the

initiating event frequency was set to the calculated frequency above.

The analyst also provided for recovery of the condensate system by

adding a basic event to the COND fault tree. This basic event COND-

RECOVERY was added under the AND gate, COND-SYS-4. This gate

then indicated that the failure of both feedwater pathways as well as

nonrecovery of the condensate system via the alternate pathway were

required to fail the condensate function.

A3-6

Attachment 3

The changes to basic events used for this model are shown on Table 2.

TABLE 2

Changes to SPAR Model Basic Events

Basic Event

Initial Value

Adjusted Value

IE-TRANS

7.0 x 10-1

6.8 x 10-2

All Other Initiators

Nominal

FALSE

MFW-AOV-CF-SGS

2.7 x 10-5

TRUE

MFW-AOV-OC-4048

7.2 x 10-6

TRUE

MFW-AOV-OC-4052

7.2 x 10-6

TRUE

MFW-SYS-AVAILABLE

0.8

1.0

MFW-SYS-UNAVAIL

0.2

FALSE

MSS-TBV-CF-TBVS

2.6 x 10-6

TRUE

COND-RECOVERY

N/A

9.3 x 10-2

The model was then quantified. The case core damage frequency (CDF)

was computed to be 4.7 x 10-7/year and the baseline CDF, using the

baseline initiating event frequency of 6.4 x 10-5/year, was computed to be

4.1 x 10-10/year. The change in CDF (CDF) was then calculated by

subtracting the baseline CDF from the case CDF. This resulted in a

CDF for the increased likelihood for a loss of instrument air of 4.7 x 10-7

over a 365-day exposure. The dominant sequences from the SPAR and

licensee models are documented in Table 3.

Table 3

Phase 3 Dominant Accident Sequences

Model

Initiating Event

Sequence

Contribution

SPAR 3.21

Loss of Instrument Air

AFW,

Condensate

4.5 x 10-7

Licensee's

Revised

Loss of Instrument Air

AFW, Failure to

Depressurize

3.1 x 10-7

A3-7

Attachment 3

External Initiating Events:

The analyst used the following methods for determining the change in risk from

external events. The change in risk from an increase in the frequency of a loss

of instrument air was estimated to be 4.2 x 10-7 for a 365-day period. The

methods used are documented below:

a.

Fire

The analyst used the San Onofre IPEEE to estimate the change in risk

resulting from internal fire. The only fire areas where risk could be

increased by the subject improperly soldered fittings would be those

containing instrument air header piping. As the limiting area, the analyst

reviewed the licensees evaluation of Fire Area 2-TB-148. The fire

ignition frequency for this area was 4.5 x 10-2/yr. The analyst assumed

that only 0.1 of the fires would grow to a size that could impact the

instrument air system (severity factor) and that about 50 percent of the

fires would cause a weakening of the improperly soldered fitting joints

without causing baseline failure of the system. Using a conditional core

damage probability of 4.2 x 10-6, the change in core damage frequency

from the subject performance deficiency related to a turbine building fire

was estimated as 9.5 x 10-9 over the 365-day exposure period.

b.

Seismic

The analyst determined that, for the subject performance deficiency to

affect the core damage frequency, a seismic event must result in a failure

of an instrument air system header fitting without otherwise affecting

instrument air system components.

To estimate the baseline seismic failure of the system, the analyst used

the seismic fragility of the air-operated valves which were the least

durable components in the system as designed. The analyst evaluated

the subject performance deficiency by determining each of the following

parameters for any seismic event producing a given range of median

acceleration "a" [SE(a)]:

1.

The frequency of the seismic event SE(a) (SE(a)) ;

2.

The probability that a system header fitting fails (PHeader-SE(a));

3.

The probability that an air-operated valve fails (P System-SE(a));

4.

The conditional change in CDP (CCDPSE(a))

The CDF for the acceleration range in question (CDFSE(a)) can then be

quantified as follows:

CDFSE(a) = SE(a) * PHeader-SE(a) * (1 - PSystem-SE(a)) * CCDPSE(a)

A3-8

Attachment 3

Given that each range a was selected by the analyst specifically to be

independent of all other ranges, the total increase in risk, CDF, can be

quantified by summing the CDFSE(a) for each range evaluated as follows:

6

CDF = 3 CDFSE(a)

a=.03

over the range of SE(a).

1.

Frequency of the Seismic Event

NRC research data indicated that seismic events of 0.05g or less have

little to no impact on internal plant equipment. The analyst assumed

that seismic events less than 0.03g do not directly affect the plant.

The analyst assumed that seismic events greater than 6.0g lead to

core damage. The analyst therefore examined seismic events in the

range of 0.03g to 6.0g.

The analyst divided that range of seismic events into segments (called

"bins" hereafter); specifically, seismic events from 0.03g to 0.1g were

binned by hundredths, seismic events from 0.1g to 1.0g were binned

by tenths, and seismic events from 1.0g to 6.0g were binned by ones.

In order to determine the frequency of a seismic event for a specific

range of ground motion (g values), the analyst used a plot provided by

the licensee and obtained values for the frequency of the seismic

event that generates a level of ground motion (in peak ground

acceleration) that exceeds the lower value in each of the bins. The

analyst then calculated the difference in these frequency of

exceedance values to obtain the frequency of seismic events for the

binned seismic event ranges.

For example, according to the San Onofre curves, the frequency of

exceedance for a 0.6g seismic event is estimated at 3.9 x 10-2/yr and a

0.7g seismic event at 3.5 x 10-2/yr. The frequency of seismic events

with median acceleration in the range of 0.6g to 0.7g [SE(0.6-0.7)]

equals the difference, or 4.0 x 10-3/yr.

2.

Probability of a Header Fitting Failure

Given that the historical header failures were the result of insufficient

solder coverage and were caused by slow degradation via air leaks,

the analyst assumed that a moderately large earthquake could result

in the failure of a leaking header fitting. Therefore, the analyst used a

median seismic fragility of a long, brittle component as an estimate of

the fragility of the 32 degraded instrument air header fittings. The

seismic fragility selected was 0.3g.

A3-9

Attachment 3

The analyst obtained data on switchyard components from the Risk

Assessment of Operating Events Handbook; Volume 2, External

Events, Revision 4, which referenced generic fragility values listed in:

<

NUREG/CR-6544, Methodology for Analyzing Precursors to

Earthquake-Initiated and Fire-Initiated Accident Sequences,

April 1998; and

<

NUREG/CR-4550, Vols 3 and 4 part 3, Analysis of Core

Damage Frequency: Surry / Peach Bottom, 1986

The references describe the mean failure probability for various

equipment using the following equation:

Pfail(a) = [ ln(a/am) / (r

2 + u

2)1/2]

Where is the standard normal cumulative distribution

function and

a =

median acceleration level of the seismic event;

am=

median of the component fragility;

r=

logarithmic standard deviation representing random

uncertainty;

u=

logarithmic standard deviation representing systematic

or modeling uncertainty.

In order to calculate the probability that a degraded fitting would fail

given a seismic event, the analyst used the following generic seismic

fragilities:

am = 0.3g

r = 0.30

u = 0.45

Using the above normal cumulative distribution function equation the

analyst determined the conditional probability of failure given a seismic

event. For each of the bins the calculation was performed substituting

for the variable "a" (median acceleration level) the acceleration levels

obtained from the bins described above. The following table shows

the results of the calculation for various acceleration levels.

Median Acceleration Level/Probability of Failure

0.03g

3.6 x 10-5

0.3g

6.1 x 10-1

1.0g

1.0

0.07g

5.2 x 10-3

0.7g

9.5 x 10-1

A3-10

Attachment 3

3.

Probability that Air-Operated Valves Fail

In order to calculate the probability that the instrument air system

would fail during a given seismic event for reasons other than

improperly soldered fittings, the analyst used the following generic

seismic fragilities for air-operated valves:

am = 3.8g

r = 0.35

u = 0.50

Using the above standard normal cumulative distribution function

equation, the analyst determined the conditional probability that the

instrument air system would fail from failure of system valves given a

seismic event for each of the bins. The calculation was performed

substituting for the variable "a" (median acceleration level) the

acceleration levels obtained from the bins described above. The

following table shows the results of the calculation for various

acceleration levels.

Median Acceleration Level/

Probability of Air-Operated Valve Failure

0.03g

7.9 x 10-15

0.3g

4.7 x 10-5

1.0g

6.4 x 10-2

0.07g

6.3 x 10-11

0.7g

3.9 x 10-3

4.

Conditional Change in Core Damage Probability

The analyst evaluated the spectrum of seismic initiators to determine

the resultant impact on the reliability and availability of mitigating

systems affecting the subject performance deficiency.

The analyst used the SPAR model, to perform the Phase 3 evaluation.

The analyst started with the model discussed above used to quantify

the change in risk from internal events. However, the analyst set the

initiating event frequency for a transient to 1.0 and all other initiating

event probabilities in the SPAR model to zero. Because of the very

narrow time windows discussed for condensate recovery, and the

added burdens on operators both emotionally and physically following

a seismic event, the analyst set the nonrecovery probability for the

condensate system to 1.0. The SPAR model showed the resultant

core damage probability as 1.02 x 10-4, which represented the value

used in the above equation.

A3-11

Attachment 3

The SPAR Model was then requantified indicating no loss of

instrument air. The CCDP for this baseline condition was 4.35 x 10-7.

Therefore, the change in core damage probability is:

CCDPSE(a) = 1.02 x 10-4 - 4.35 x 10-7 = 1.02 x 10-4

Phase 3 Seismic Results

Given the assumptions previously discussed, the total increase in core

damage frequency was estimated to be about 4.1 x 10-7 for seismic events

ranging from 0.03g to 6.0g.

c.

Winds, Floods, and Other External Events

The analyst reviewed the IPEEE and determined that no other credible

scenarios initiated by high winds, floods, fire, and other external events could

initiate a failure of the degraded instrument air header fittings. Therefore, the

analyst concluded that external events other than internal fires and seismic

events were not significant contributors to risk for this finding.

Risk Contribution from Large Early Release Frequency (LERF):

Using IMC 0609 Appendix H, the SRA determined that this was a Type A finding for a

large dry containment. For PWR plants with large dry containments, only findings

related to accident categories ISLOCA and SGTR have the potential to impact LERF.

In addition, an important insight from the IPE program and other PRAs is that the

conditional probability of early containment failure is less than 0.1 for core damage

scenarios that leave the RCS at high pressure (>250 psi) at the time of reactor vessel

breach. Since this finding is not related to ISLOCA or SGTR, and the core damage

scenarios for this finding leave the RCS at high pressure, the analyst concluded that

LERF is not a significant contributor to the risk associated with this finding.