ML17342B421: Difference between revisions
StriderTol (talk | contribs) (Created page by program invented by StriderTol) |
StriderTol (talk | contribs) (StriderTol Bot change) |
||
| Line 17: | Line 17: | ||
=Text= | =Text= | ||
{{#Wiki_filter:Florida | {{#Wiki_filter:ENCLOSURE 1 | ||
Docket No. 50-250 License No. DPR-31 EA 89-47 During the Nuclear Regulatory Commission (NRC) inspection conducted on January 17-20, 1989, a violation of NRC requirements was identified. | 0~ | ||
Criterion | 0 Florida Power and Light Company Tur'key Point Plant Docket No. 50-250 License No. | ||
Section 5.4.8 of Procedure | DPR-31 EA 89-47 During the Nuclear Regulatory Commission (NRC) inspection conducted on January 17-20, | ||
Emergency Procedure | : 1989, a violation of NRC requirements was identified. | ||
In accordance with the "General Statement of Policy and Procedure for NRC Enforcement Actions," | |||
10 CFR Part 2, Appendix C (1988), | |||
the violation is listed below: | |||
Criterion V of Appendix 8 to 10 CFR Part 50, as implemented by the licensee's accepted Quality Assurance Program (FPL QAR-1-76A, dated June 10, 1987), | |||
requires that activities affecting quality be in accordance with approved procedures. | |||
Section 5.4.8 of Procedure QP 5. 1 (Revision | |||
: 3) of the licensee's Quality Assurance Manual requires that procedures be developed to implement the Plant Emergency Plan. | |||
Emergency Procedure 20101 (Duties of the Emergency Coordinator) specifies an Alert declaration upon determination of Reactor Coolant System (RCS) leakage exceeding 50 gpm, followed by notification to the State of Florida within 15 minutes and the NRC within 60 minutes. | |||
Contrary to the above, on January 7, 1989, the licensee failed to promptly classify an event involving Unit 3 RCS leakage greater thah 50 gpm and to make timely notification to the State of Florida and the NRC. | Contrary to the above, on January 7, 1989, the licensee failed to promptly classify an event involving Unit 3 RCS leakage greater thah 50 gpm and to make timely notification to the State of Florida and the NRC. | ||
This is | This is a Severity Level IV violation (Supplement VIII). | ||
Pursuant to the provisions of 10 CFR 2.201, Florida Power and Light Company is hereby required to submit a written statement or explanation to the Director, Office of Enforcement, U.S. Nuclear Regulatory Commission, within 30 days of the date of this Notice. This reply should be clearly marked as a "Reply to a Notice of Violation" and should include: ( 1) admission or denial of the violation, (2) the reasons for the violation | Pursuant to the provisions of 10 CFR 2.201, Florida Power and Light Company is hereby required to submit a written statement or explanation to the Director, Office of Enforcement, U.S. | ||
Nuclear Regulatory Commission, within 30 days of the date of this Notice. | |||
This reply should be clearly marked as a "Reply to a Notice of Violation" and should include: | |||
( 1) admission or denial of the violation, (2) the reasons for the violation if admitted, (3) the corrective steps that have been taken and the results | |||
: achieved, (4) the corrective steps which will be taken to avoid further violations, and (5) the date when full compliance will be achieved. | |||
If an adequate reply is not received within the time specified in this Notice, an order may be issued to show cause why the 8903090099 890224 PDR ADOCN, 05000250 G | |||
PNU | |||
Florida | Florida Power and Light Company Turkey Point Plant Docket Nos. | ||
FOR THE NUCLEAR REGULATORY COMMISSlON | 50-250, 50-251 License Nos. | ||
DPR-31, DPR-41 license should not be modified, suspended, or revoked or why such other action as may be proper should not be taken. | |||
FOR THE NUCLEAR REGULATORY COMMISSlON Dated at Atlanta, Georgia this day of 1989 lgo m | |||
L rnst cting Regional Administrator}} | |||
Latest revision as of 11:49, 7 January 2025
| ML17342B421 | |
| Person / Time | |
|---|---|
| Site: | Shoreham File:Long Island Lighting Company icon.png |
| Issue date: | 03/03/1988 |
| From: | Mark Miller KIRKPATRICK & LOCKHART, SUFFOLK COUNTY, NY |
| To: | NRC OFFICE OF THE GENERAL COUNSEL (OGC) |
| References | |
| CON-#188-5755 OL-3, NUDOCS 8803090099 | |
| Download: ML17342B421 (4) | |
Text
ENCLOSURE 1
0~
0 Florida Power and Light Company Tur'key Point Plant Docket No. 50-250 License No.
DPR-31 EA 89-47 During the Nuclear Regulatory Commission (NRC) inspection conducted on January 17-20,
- 1989, a violation of NRC requirements was identified.
In accordance with the "General Statement of Policy and Procedure for NRC Enforcement Actions,"
10 CFR Part 2, Appendix C (1988),
the violation is listed below:
Criterion V of Appendix 8 to 10 CFR Part 50, as implemented by the licensee's accepted Quality Assurance Program (FPL QAR-1-76A, dated June 10, 1987),
requires that activities affecting quality be in accordance with approved procedures.
Section 5.4.8 of Procedure QP 5. 1 (Revision
- 3) of the licensee's Quality Assurance Manual requires that procedures be developed to implement the Plant Emergency Plan.
Emergency Procedure 20101 (Duties of the Emergency Coordinator) specifies an Alert declaration upon determination of Reactor Coolant System (RCS) leakage exceeding 50 gpm, followed by notification to the State of Florida within 15 minutes and the NRC within 60 minutes.
Contrary to the above, on January 7, 1989, the licensee failed to promptly classify an event involving Unit 3 RCS leakage greater thah 50 gpm and to make timely notification to the State of Florida and the NRC.
This is a Severity Level IV violation (Supplement VIII).
Pursuant to the provisions of 10 CFR 2.201, Florida Power and Light Company is hereby required to submit a written statement or explanation to the Director, Office of Enforcement, U.S.
Nuclear Regulatory Commission, within 30 days of the date of this Notice.
This reply should be clearly marked as a "Reply to a Notice of Violation" and should include:
( 1) admission or denial of the violation, (2) the reasons for the violation if admitted, (3) the corrective steps that have been taken and the results
- achieved, (4) the corrective steps which will be taken to avoid further violations, and (5) the date when full compliance will be achieved.
If an adequate reply is not received within the time specified in this Notice, an order may be issued to show cause why the 8903090099 890224 PDR ADOCN, 05000250 G
PNU
Florida Power and Light Company Turkey Point Plant Docket Nos.
50-250, 50-251 License Nos.
DPR-31, DPR-41 license should not be modified, suspended, or revoked or why such other action as may be proper should not be taken.
FOR THE NUCLEAR REGULATORY COMMISSlON Dated at Atlanta, Georgia this day of 1989 lgo m
L rnst cting Regional Administrator