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{{#Wiki_filter:July 18, 2018
{{#Wiki_filter:July 18, 2018  
Mr. William F. Maguire, Site Vice President
Entergy Operations, Inc.
River Bend Station
5485 U.S. Highway 61N
Mr. William F. Maguire, Site Vice President  
St. Francisville, LA 70775
Entergy Operations, Inc.  
SUBJECT:       RIVER BEND STATION - NRC BASELINE INSPECTION REPORT
River Bend Station  
                05000458/2018012
5485 U.S. Highway 61N  
Dear Mr. Maguire:
St. Francisville, LA 70775  
On July 16, 2018, the U.S. Nuclear Regulatory Commission (NRC) completed a baseline
inspection at your River Bend Station, Unit 1. On May 31 and July 16, 2018, the NRC
SUBJECT:  
inspection team discussed the results of this inspection with you and other members of your
RIVER BEND STATION - NRC BASELINE INSPECTION REPORT  
staff. The results of this inspection are documented in the enclosed report.
05000458/2018012  
NRC inspectors documented five findings of very low safety significance (Green) in this report.
Four of these findings involved violations of NRC requirements. Additionally, NRC inspectors
Dear Mr. Maguire:  
documented two violations that were determined to be Severity Level IV under the traditional
enforcement process. The NRC is treating these violations as non-cited violations (NCVs)
On July 16, 2018, the U.S. Nuclear Regulatory Commission (NRC) completed a baseline  
consistent with Section 2.3.2.a of the NRC Enforcement Policy.
inspection at your River Bend Station, Unit 1. On May 31 and July 16, 2018, the NRC  
If you contest the violations or significance of these NCVs, you should provide a response within
inspection team discussed the results of this inspection with you and other members of your  
30 days of the date of this inspection report, with the basis for your denial, to the U.S. Nuclear
staff. The results of this inspection are documented in the enclosed report.  
Regulatory Commission, ATTN: Document Control Desk, Washington, DC 20555-0001; with
copies to the Regional Administrator, Region IV; the Director, Office of Enforcement; and the
NRC inspectors documented five findings of very low safety significance (Green) in this report.
NRC resident inspector at the River Bend Station.
Four of these findings involved violations of NRC requirements. Additionally, NRC inspectors  
If you disagree with a cross-cutting aspect assignment in this report, you should provide a
documented two violations that were determined to be Severity Level IV under the traditional  
response within 30 days of the date of this inspection report, with the basis for your
enforcement process. The NRC is treating these violations as non-cited violations (NCVs)  
disagreement, to the U.S. Nuclear Regulatory Commission, ATTN: Document Control Desk,
consistent with Section 2.3.2.a of the NRC Enforcement Policy.  
Washington, DC 20555-0001; with copies to the Regional Administrator, Region IV; and the
NRC resident inspector at the River Bend Station.
If you contest the violations or significance of these NCVs, you should provide a response within  
30 days of the date of this inspection report, with the basis for your denial, to the U.S. Nuclear  
Regulatory Commission, ATTN: Document Control Desk, Washington, DC 20555-0001; with  
copies to the Regional Administrator, Region IV; the Director, Office of Enforcement; and the  
NRC resident inspector at the River Bend Station.  
If you disagree with a cross-cutting aspect assignment in this report, you should provide a  
response within 30 days of the date of this inspection report, with the basis for your  
disagreement, to the U.S. Nuclear Regulatory Commission, ATTN: Document Control Desk,  
Washington, DC 20555-0001; with copies to the Regional Administrator, Region IV; and the  
NRC resident inspector at the River Bend Station.  


W. Maguire                                       2
W. Maguire  
This letter, its enclosure, and your response (if any) will be made available for public inspection
2  
and copying at http://www.nrc.gov/reading-rm/adams.html and at the NRC Public Document
This letter, its enclosure, and your response (if any) will be made available for public inspection  
Room in accordance with 10 CFR 2.390, Public Inspections, Exemptions, Requests for
and copying at http://www.nrc.gov/reading-rm/adams.html and at the NRC Public Document  
Withholding.
Room in accordance with 10 CFR 2.390, Public Inspections, Exemptions, Requests for  
                                                Sincerely,
Withholding.  
                                                /RA/
                                                Jason W. Kozal, Chief
Sincerely,  
                                                Project Branch C
                                                Division of Reactor Projects
Docket No. 50-458
/RA/  
License No. NPF-47
Enclosure:
Jason W. Kozal, Chief  
Inspection Report 05000458/2018012
Project Branch C  
w/ Attachment: Documents Reviewed
Division of Reactor Projects  
Docket No. 50-458  
License No. NPF-47  
Enclosure:  
Inspection Report 05000458/2018012  
w/ Attachment: Documents Reviewed  


                          U.S. NUCLEAR REGULATORY COMMISSION
                                        Inspection Report
Docket Number:         05000458
License Number:       NPF-47
Enclosure
Report Number:         05000458/2018012
U.S. NUCLEAR REGULATORY COMMISSION  
Enterprise Identifier: I-2018-012-0015
Inspection Report  
Licensee:             Entergy Operations, Inc.
Facility:             River Bend Station
Location:             Saint Francisville, Louisiana
Docket Number:
Inspection Dates:     February 1, 2018 to July 16, 2018.
05000458  
Inspectors:           J. Sowa, Senior Resident Inspector
                      J. Drake, Senior Reactor Inspector
                      C. Young, Senior Project Engineer
License Number:  
                      M. OBanion, Resident Inspector (Acting)
NPF-47  
                      B. Parks, Resident Inspector
Approved By:           J. Kozal, Chief, Branch C
                      Division of Reactor Projects
Report Number:  
                                                                Enclosure
05000458/2018012  
Enterprise Identifier: I-2018-012-0015  
Licensee:  
Entergy Operations, Inc.  
Facility:  
River Bend Station  
Location:  
Saint Francisville, Louisiana  
Inspection Dates:  
February 1, 2018 to July 16, 2018.  
Inspectors:  
J. Sowa, Senior Resident Inspector  
J. Drake, Senior Reactor Inspector  
C. Young, Senior Project Engineer  
M. OBanion, Resident Inspector (Acting)  
B. Parks, Resident Inspector
Approved By:  
J. Kozal, Chief, Branch C  
Division of Reactor Projects  


                                            SUMMARY
The U.S. Nuclear Regulatory Commission (NRC) continued monitoring the licensees
performance by conducting a baseline inspection at River Bend Station in accordance with the
2
Reactor Oversight Process. The Reactor Oversight Process is the NRCs program for
overseeing the safe operation of commercial nuclear power reactors. Refer to
SUMMARY  
https://www.nrc.gov/reactors/operating/oversight.html for more information. Findings and
The U.S. Nuclear Regulatory Commission (NRC) continued monitoring the licensees  
violations being considered in the NRCs assessment are summarized in the tables below.
performance by conducting a baseline inspection at River Bend Station in accordance with the  
                                  List of Findings and Violations
Reactor Oversight Process. The Reactor Oversight Process is the NRCs program for  
  Failure to Identify and Correct a Broken Feedwater Chemistry Probe
overseeing the safe operation of commercial nuclear power reactors. Refer to  
  Cornerstone       Significance                                         Cross-cutting     Report
https://www.nrc.gov/reactors/operating/oversight.html for more information. Findings and  
                                                                          Aspect            Section
violations being considered in the NRCs assessment are summarized in the tables below.  
  Barrier           Green                                                 None              71152 -
  Integrity        NCV 05000458/2018012-02                                                 Problem
List of Findings and Violations  
                    Closed                                                                  Identification
Failure to Identify and Correct a Broken Feedwater Chemistry Probe  
                                                                                            and
Cornerstone  
                                                                                            Resolution
Significance  
  Two examples of a self-revealed non-cited violation (NCV) of 10 CFR Part 50, Appendix B,
Cross-cutting  
  Criterion XVI, Corrective Action, were identified for the licensees failure to identify that a
Aspect
  broken chemistry probe in the feedwater system had the potential to cause an adverse impact
Report  
  on plant safety, and promptly implement appropriate measures to address that condition.
Section  
  Failure to Provide Adequate Procedures for Post-Scram Recovery
Barrier  
  Cornerstone       Significance                                         Cross-cutting     Report
Integrity
                                                                          Aspect            Section
Green  
  Mitigating       Green                                                 None              71111.18 -
NCV 05000458/2018012-02  
  Systems          NCV 05000458/2018012-06                                                 Plant
Closed
                    Closed                                                                  Modifications
None
  The inspectors reviewed a self-revealed, non-cited violation of Technical Specification 5.4.1.a for
71152 - 
  the licensees failure to establish, implement and maintain a procedure required by Regulatory
Problem  
  Guide 1.33, Revision 2, Appendix A, dated February 1978. Specifically, Procedure OSP-0053,
Identification  
  Emergency and Transient Response Support Procedure, Revision 22, which is required by
and  
  Regulatory Guide 1.33, inappropriately directed operations personnel to establish feedwater flow
Resolution  
  to the reactor pressure vessel using the main feedwater regulating valve as part of the post-
Two examples of a self-revealed non-cited violation (NCV) of 10 CFR Part 50, Appendix B,  
  scram actions. This resulted in the main feedwater regulating valves being operated outside
Criterion XVI, Corrective Action, were identified for the licensees failure to identify that a  
  their design limits. This resulted in catastrophic failure of the main feedwater regulating valve
broken chemistry probe in the feedwater system had the potential to cause an adverse impact  
  variseals and subsequent damage to multiple fuel assemblies.
on plant safety, and promptly implement appropriate measures to address that condition.  
                                                  2
Failure to Provide Adequate Procedures for Post-Scram Recovery  
Cornerstone  
Significance  
Cross-cutting  
Aspect
Report  
Section  
Mitigating  
Systems
Green  
NCV 05000458/2018012-06  
Closed
None
71111.18 -
Plant  
Modifications  
The inspectors reviewed a self-revealed, non-cited violation of Technical Specification 5.4.1.a for  
the licensees failure to establish, implement and maintain a procedure required by Regulatory  
Guide 1.33, Revision 2, Appendix A, dated February 1978. Specifically, Procedure OSP-0053,  
Emergency and Transient Response Support Procedure, Revision 22, which is required by  
Regulatory Guide 1.33, inappropriately directed operations personnel to establish feedwater flow  
to the reactor pressure vessel using the main feedwater regulating valve as part of the post-
scram actions. This resulted in the main feedwater regulating valves being operated outside  
their design limits. This resulted in catastrophic failure of the main feedwater regulating valve  
variseals and subsequent damage to multiple fuel assemblies.  


Failure to Develop an Adequate Operational Decision-Making Issue for Compensatory Measures
Related to a Degraded Condition of the Feedwater System Sparger Nozzles
Cornerstone       Significance                                       Cross-cutting Report Section
3
                                                                    Aspect
Mitigating        Green                                             [H.9] -         71111.15 -
Failure to Develop an Adequate Operational Decision-Making Issue for Compensatory Measures  
Systems          NCV 05000458/2018012-05                            Human          Operability
Related to a Degraded Condition of the Feedwater System Sparger Nozzles  
                  Closed                                            Performance, Determinations
Cornerstone  
                                                                    Training        and
Significance  
                                                                                    Functionality
Cross-cutting  
                                                                                    Assessment
Aspect
The inspectors identified a Green non-cited violation of 10 CFR Part 50, Appendix B, Criterion V,
Report Section  
Instructions, Procedures, and Drawings, for the failure to develop an adequate Operational
Mitigating
Systems
Green  
NCV 05000458/2018012-05
Closed
[H.9] -  
Human
Performance,
Training
71111.15 -  
Operability  
Determinations  
and  
Functionality  
Assessment  
The inspectors identified a Green non-cited violation of 10 CFR Part 50, Appendix B, Criterion V,  
Instructions, Procedures, and Drawings, for the failure to develop an adequate Operational  
Decision-Making Issue (ODMI) document per Procedure EN-OP-111, Operational Decision-
Decision-Making Issue (ODMI) document per Procedure EN-OP-111, Operational Decision-
Making Issue Process. Specifically, the licensee failed to develop an ODMI that provided
Making Issue Process. Specifically, the licensee failed to develop an ODMI that provided  
adequate guidance to the operators for safely operating the plant with degraded feedwater
adequate guidance to the operators for safely operating the plant with degraded feedwater  
sparger nozzles.
sparger nozzles.  
Failure to Establish Procedural Guidance for Determining Core Flow During Unanticipated
Single Loop Operations
Failure to Establish Procedural Guidance for Determining Core Flow During Unanticipated  
Cornerstone       Significance                                         Cross-cutting Report
Single Loop Operations  
                                                                      Aspect          Section
Cornerstone  
Initiating       Green                                               [P.3] -         71153 -
Significance  
Events            NCV 05000458/2018012-03                              Problem        Follow-up of
Cross-cutting  
                  Closed                                              Identification Events and
Aspect
                                                                      and            Notices of
Report  
                                                                      Resolution,    Enforcement
Section  
                                                                      Resolution      Discretion
Initiating  
The inspectors reviewed a self-revealed, non-cited violation of 10 CFR Part 50 Appendix B,
Events
Criterion V, Instructions, Procedures, and Drawings, for the licensees failure to establish
Green  
appropriate instructions in the abnormal operating procedure for thermal hydraulic instabilities.
NCV 05000458/2018012-03
Specifically, the procedural step for determining core flow when in single loop operations at low
Closed
power did not provide appropriate instructions to operators. As a result, station personnel could
[P.3] -  
not conclusively determine core flow and inserted a manual reactor scram.
Problem
Failure to Perform 10 CFR 50.59 Evaluation for Main Feedwater System Sparger Nozzle
Identification
Damage
and
Cornerstone       Significance                                         Cross-cutting Report
Resolution,
                                                                      Aspect          Section
Resolution
None             SL-IV                                               None            71111.18 -
71153 -
                  NCV 05000458/2018012-07                                             Plant
Follow-up of  
                  Closed                                                              Modifications
Events and  
The inspectors identified a Severity Level IV non-cited violation of 10 CFR 50.59, Changes,
Notices of  
Tests, and Experiments, for the licensees failure to provide a written safety evaluation for the
Enforcement  
determination that operation with compensatory measures for damaged feedwater sparger
Discretion  
nozzles did not require a license amendment pursuant to 10 CFR 50.90, Application for
The inspectors reviewed a self-revealed, non-cited violation of 10 CFR Part 50 Appendix B,  
amendment of license, construction permit, or early site permit. Specifically, the licensee failed
Criterion V, Instructions, Procedures, and Drawings, for the licensees failure to establish  
to recognize that compensatory measures prohibiting operation in single loop conditions
appropriate instructions in the abnormal operating procedure for thermal hydraulic instabilities.
required technical specification changes, and as such required prior NRC approval.
Specifically, the procedural step for determining core flow when in single loop operations at low  
                                              3
power did not provide appropriate instructions to operators. As a result, station personnel could  
not conclusively determine core flow and inserted a manual reactor scram.  
Failure to Perform 10 CFR 50.59 Evaluation for Main Feedwater System Sparger Nozzle  
Damage  
Cornerstone  
Significance  
Cross-cutting  
Aspect
Report  
Section  
None  
SL-IV  
NCV 05000458/2018012-07  
Closed
None
71111.18 -
Plant  
Modifications  
The inspectors identified a Severity Level IV non-cited violation of 10 CFR 50.59, Changes,  
Tests, and Experiments, for the licensees failure to provide a written safety evaluation for the  
determination that operation with compensatory measures for damaged feedwater sparger  
nozzles did not require a license amendment pursuant to 10 CFR 50.90, Application for  
amendment of license, construction permit, or early site permit. Specifically, the licensee failed  
to recognize that compensatory measures prohibiting operation in single loop conditions  
required technical specification changes, and as such required prior NRC approval.  


Failure to Conduct Adequate Transient Snap Shot Assessment Following Recirculation Pump
Trip
Cornerstone       Significance                                       Cross-cutting Report
4
                                                                      Aspect            Section
Initiating       Green                                               None              71152 -
Failure to Conduct Adequate Transient Snap Shot Assessment Following Recirculation Pump  
Events            FIN 05000458/2018012-01                                               Problem
Trip  
                  Closed                                                                Identification
Cornerstone  
                                                                                        and
Significance  
                                                                                        Resolution
Cross-cutting  
The inspectors identified a finding for the licensees failure to adequately validate simulator
Aspect
response during a transient snap shot assessment following an unexpected trip of reactor
Report  
recirculation pump A on December 19, 2012.
Section  
Failure to Submit a Licensee Event Report for a Manual Scram
Initiating  
Cornerstone       Significance                                         Cross-cutting   Report
Events
                                                                      Aspect          Section
Green  
None             SL-IV                                               None            71153 -
FIN 05000458/2018012-01  
                  NCV 05000458/2018012-04                                               Follow-up of
Closed
                  Closed                                                                Events and
None
                                                                                        Notices of
71152 -
                                                                                        Enforcement
Problem  
                                                                                        Discretion
Identification  
The inspectors identified a Severity Level IV non-cited violation of 10 CFR 50.73, Licensee
and  
Event Report System, for the licensees failure to submit a required licensee event report (LER).
Resolution  
Specifically, on February 1, 2018, after an unexpected trip of the recirculation pump B, the
The inspectors identified a finding for the licensees failure to adequately validate simulator  
licensee initiated a manual scram of the reactor that was not part of a preplanned sequence and
response during a transient snap shot assessment following an unexpected trip of reactor  
failed to submit an LER within 60 days.
recirculation pump A on December 19, 2012.  
                                                4
Failure to Submit a Licensee Event Report for a Manual Scram  
Cornerstone  
Significance  
Cross-cutting  
Aspect
Report  
Section  
None  
SL-IV  
NCV 05000458/2018012-04  
Closed
None
71153 -
Follow-up of  
Events and  
Notices of  
Enforcement  
Discretion  
The inspectors identified a Severity Level IV non-cited violation of 10 CFR 50.73, Licensee  
Event Report System, for the licensees failure to submit a required licensee event report (LER).
Specifically, on February 1, 2018, after an unexpected trip of the recirculation pump B, the  
licensee initiated a manual scram of the reactor that was not part of a preplanned sequence and  
failed to submit an LER within 60 days.  


INSPECTION SCOPES
Inspections were conducted using the appropriate portions of the inspection procedures (IPs) in
effect at the beginning of the inspection unless otherwise noted. Currently approved IPs with
5
INSPECTION SCOPES  
Inspections were conducted using the appropriate portions of the inspection procedures (IPs) in  
effect at the beginning of the inspection unless otherwise noted. Currently approved IPs with  
their attached revision histories are located on the public website at http://www.nrc.gov/reading-
their attached revision histories are located on the public website at http://www.nrc.gov/reading-
rm/doc-collections/insp-manual/inspection-procedure/index.html. Samples were declared
rm/doc-collections/insp-manual/inspection-procedure/index.html. Samples were declared  
complete when the IP requirements most appropriate to the inspection activity were met
complete when the IP requirements most appropriate to the inspection activity were met  
consistent with Inspection Manual Chapter (IMC) 2515, Light-Water Reactor Inspection
consistent with Inspection Manual Chapter (IMC) 2515, Light-Water Reactor Inspection  
Program - Operations Phase. The inspectors reviewed selected procedures and records,
Program - Operations Phase.   The inspectors reviewed selected procedures and records,  
observed activities, and interviewed personnel to assess licensee performance and compliance
observed activities, and interviewed personnel to assess licensee performance and compliance  
with Commission rules and regulations, license conditions, site procedures, and standards.
with Commission rules and regulations, license conditions, site procedures, and standards.  
REACTOR SAFETY
71111.15Operability Determinations and Functionality Assessments (1 Sample)
REACTOR SAFETY  
    The inspectors evaluated the following operability determinations and functionality
71111.15Operability Determinations and Functionality Assessments (1 Sample)  
    assessments:
The inspectors evaluated the following operability determinations and functionality  
    (1) Review of Operational Decision-Making Issue (ODMI) associated with damaged
assessments:  
        feedwater sparger on February 8, 2018
71111.18Plant Modifications (2 Samples)
(1) Review of Operational Decision-Making Issue (ODMI) associated with damaged  
    The inspectors evaluated the following temporary or permanent modifications:
feedwater sparger on February 8, 2018  
    (1) OSP-0053, Emergency And Transient Response Support Procedure, following
        decision to control reactor vessel level with main feedwater regulating valves during
71111.18Plant Modifications (2 Samples)  
        post-scram operations
The inspectors evaluated the following temporary or permanent modifications:  
    (2) Review of plant operation following modification to feedwater sparger nozzles 7 and 8
OTHER ACTIVITIES - BASELINE
(1) OSP-0053, Emergency And Transient Response Support Procedure, following  
71152Problem Identification and Resolution
decision to control reactor vessel level with main feedwater regulating valves during  
    Annual Follow-up of Selected Issues (3 Samples)
post-scram operations  
    The inspectors reviewed the licensees implementation of its corrective action program
    related to the following issues:
(2) Review of plant operation following modification to feedwater sparger nozzles 7 and 8  
    (1) Review of 1) simulator modelling of core parameters during a recirculation pump trip at
        low power and 2) licensed operator training associated with single loop operations at low
OTHER ACTIVITIES - BASELINE  
        power
71152Problem Identification and Resolution  
    (2) Actions to address a broken isokinetic chemistry sampling probe in the feedwater
Annual Follow-up of Selected Issues (3 Samples)  
        system
The inspectors reviewed the licensees implementation of its corrective action program  
    (3) Actions to address fuel failures caused by debris material in the reactor vessel
related to the following issues:  
                                                  5
(1) Review of 1) simulator modelling of core parameters during a recirculation pump trip at  
low power and 2) licensed operator training associated with single loop operations at low  
power  
(2) Actions to address a broken isokinetic chemistry sampling probe in the feedwater  
system  
(3) Actions to address fuel failures caused by debris material in the reactor vessel  


71153Follow-up of Events and Notices of Enforcement Discretion
    Personnel Performance (1 Sample)
    (1) The inspectors evaluated operator response to the unexpected trip of the reactor
6
        recirculation pump B on February 1, 2018.
INSPECTION RESULTS
71153Follow-up of Events and Notices of Enforcement Discretion  
Failure to Identify and Correct a Broken Feedwater System Chemistry Probe
Personnel Performance (1 Sample)  
Cornerstone       Significance                                   Cross-cutting     Report
(1) The inspectors evaluated operator response to the unexpected trip of the reactor  
                                                                    Aspect            Section
recirculation pump B on February 1, 2018.  
Barrier           Green                                           None              71152 -
Integrity          NCV 05000458/2018012-02                                           Problem
INSPECTION RESULTS  
                    Closed                                                            Identification
Failure to Identify and Correct a Broken Feedwater System Chemistry Probe  
                                                                                      and
Cornerstone  
                                                                                      Resolution
Significance  
Two examples of a self-revealed Green finding and associated NCV of 10 CFR Part 50,
Cross-cutting  
Appendix B, Criterion XVI, were identified for the licensees failure to identify that a broken
Aspect
chemistry probe in the feedwater system had the potential to cause an adverse impact on
Report  
plant safety, and promptly implement appropriate measures to address that condition.
Section  
Description:
Barrier  
  In 1999, the licensee initiated Condition Report CR-RBS-1999-1011 to document that an
Integrity
isokinetic chemistry sample probe was found to be missing from its installed location in the
Green  
feedwater system, having broken off in the system. Following unsuccessful attempts to
NCV 05000458/2018012-02  
locate and remove the missing probe, the licensee performed evaluation ER-99-0539 to
Closed
evaluate the potential impact of the missing probe on the continued operation and function of
None
feedwater system components. This evaluation concluded that the missing probe remaining
71152 -
in the system would not present any hazard to any feedwater system components, and would
Problem  
have no adverse effect on continued operation. This conclusion was based, in part, on a
Identification  
calculation showing that feedwater flow would not have enough energy to levitate the probe
and  
past a 20-foot vertical riser portion of the system, and therefore would not have the potential
Resolution  
to enter a feedwater sparger in the reactor vessel downstream of the vertical riser. Another
Two examples of a self-revealed Green finding and associated NCV of 10 CFR Part 50,  
calculation showed that the impact energy of the loose probe on any feedwater components
Appendix B, Criterion XVI, were identified for the licensees failure to identify that a broken  
would be negligible.
chemistry probe in the feedwater system had the potential to cause an adverse impact on  
  In March 2004, the NRC issued Information Notice (IN) 2004-06, Loss of Feedwater
plant safety, and promptly implement appropriate measures to address that condition.  
Isokinetic Sampling Probes at Dresden Units 2 and 3 (ADAMS Accession No.
Description:  
ML040711214). The IN discussed that broken probes had been discovered at five other
   
stations from 1990 to 2001, and further described the conditions discovered at Dresden
In 1999, the licensee initiated Condition Report CR-RBS-1999-1011 to document that an  
Nuclear Power Station (Dresden), Units 2 and 3. In 2003, three holes in a feedwater sparger
isokinetic chemistry sample probe was found to be missing from its installed location in the  
at Dresden Unit 2 were discovered, along with the missing feedwater probe in the sparger,
feedwater system, having broken off in the system. Following unsuccessful attempts to  
which had apparently caused the damage. Two probes were discovered to be in a feedwater
locate and remove the missing probe, the licensee performed evaluation ER-99-0539 to  
sparger in Dresden Unit 3, with no damage to the sparger having occurred yet. These
evaluate the potential impact of the missing probe on the continued operation and function of  
conditions demonstrated that not only could the probes be transported to the feedwater
feedwater system components. This evaluation concluded that the missing probe remaining  
spargers in the reactor vessel, but that they could potentially damage the spargers. The
in the system would not present any hazard to any feedwater system components, and would  
licensees evaluation of this operating experience concluded that, since the broken probe at
have no adverse effect on continued operation. This conclusion was based, in part, on a  
River Bend had been replaced with a probe of a design not susceptible to the same failure,
calculation showing that feedwater flow would not have enough energy to levitate the probe  
no further action was needed. The licensee failed to address the potential impacts of the
past a 20-foot vertical riser portion of the system, and therefore would not have the potential  
adverse condition of the broken probe that remained loose in the feedwater system.
to enter a feedwater sparger in the reactor vessel downstream of the vertical riser. Another  
                                                  6
calculation showed that the impact energy of the loose probe on any feedwater components  
would be negligible.  
   
In March 2004, the NRC issued Information Notice (IN) 2004-06, Loss of Feedwater  
Isokinetic Sampling Probes at Dresden Units 2 and 3 (ADAMS Accession No.  
ML040711214). The IN discussed that broken probes had been discovered at five other  
stations from 1990 to 2001, and further described the conditions discovered at Dresden  
Nuclear Power Station (Dresden), Units 2 and 3. In 2003, three holes in a feedwater sparger  
at Dresden Unit 2 were discovered, along with the missing feedwater probe in the sparger,  
which had apparently caused the damage. Two probes were discovered to be in a feedwater  
sparger in Dresden Unit 3, with no damage to the sparger having occurred yet. These  
conditions demonstrated that not only could the probes be transported to the feedwater  
spargers in the reactor vessel, but that they could potentially damage the spargers. The  
licensees evaluation of this operating experience concluded that, since the broken probe at  
River Bend had been replaced with a probe of a design not susceptible to the same failure,  
no further action was needed. The licensee failed to address the potential impacts of the  
adverse condition of the broken probe that remained loose in the feedwater system.  


In 2011, the licensee documented an evaluation of a similar condition that had been
discovered at Brunswick Steam Electric Plant, Unit 2, where a feedwater sample probe was
discovered inside a feedwater sparger. The licensees evaluation of this operating
7
experience concluded that the current design (i.e. the probe that replaced the previous
broken probe) was not susceptible to this kind of failure. The licensee again failed to address
In 2011, the licensee documented an evaluation of a similar condition that had been  
the impact of the previous broken probe that remained in the system, given that its potential
discovered at Brunswick Steam Electric Plant, Unit 2, where a feedwater sample probe was  
to be transported into a feedwater sparger in the reactor vessel had been shown.
discovered inside a feedwater sparger. The licensees evaluation of this operating  
In January 2018, the licensee discovered damage in the form of two holes in feedwater
experience concluded that the current design (i.e. the probe that replaced the previous  
sparger nozzles in the reactor vessel, with the broken probe protruding from one of the holes
broken probe) was not susceptible to this kind of failure. The licensee again failed to address  
in the direction of the other. The broken probe remaining in the feedwater system resulted in
the impact of the previous broken probe that remained in the system, given that its potential  
potential adverse impacts on the reactor vessel wall due to impingement of feedwater flow
to be transported into a feedwater sparger in the reactor vessel had been shown.  
through the holes in the damaged sparger, as well as potential adverse impacts on the
integrity of fuel cladding due to the introduction of foreign material (pieces of the feedwater
In January 2018, the licensee discovered damage in the form of two holes in feedwater  
sparger and chemistry probe) in the reactor vessel.
sparger nozzles in the reactor vessel, with the broken probe protruding from one of the holes  
Corrective Actions: The broken probe was removed from the system. The licensee
in the direction of the other. The broken probe remaining in the feedwater system resulted in  
performed evaluations to identify plant operational limitations to ensure that adverse impacts
potential adverse impacts on the reactor vessel wall due to impingement of feedwater flow  
to reactor pressure vessel wall integrity from additional holes in a feedwater sparger are
through the holes in the damaged sparger, as well as potential adverse impacts on the  
minimized. The licensee also issued an action to perform a review of historical loose parts
integrity of fuel cladding due to the introduction of foreign material (pieces of the feedwater  
evaluations to add to tracking mechanisms and ensure adequacy of previous evaluations.
sparger and chemistry probe) in the reactor vessel.  
Corrective Action Reference: CR-RBS-2018-0294, CR-RBS-2018-0613, and
CR-RBS-2017-2828.
Corrective Actions: The broken probe was removed from the system. The licensee  
Performance Assessment:
performed evaluations to identify plant operational limitations to ensure that adverse impacts  
Performance Deficiency: The licensees failure on two occasions to identify a broken
to reactor pressure vessel wall integrity from additional holes in a feedwater sparger are  
chemistry probe in the feedwater system had the potential to cause an adverse impact on
minimized. The licensee also issued an action to perform a review of historical loose parts  
plant safety and to promptly implement appropriate measures to address that condition was a
evaluations to add to tracking mechanisms and ensure adequacy of previous evaluations.  
performance deficiency.
Screening: The inspectors determined the performance deficiency was more than minor
Corrective Action Reference: CR-RBS-2018-0294, CR-RBS-2018-0613, and  
because it was associated with the Cladding Performance, as well as the RCS Equipment
CR-RBS-2017-2828.  
and Barrier Performance, attributes of the Barrier Integrity Cornerstone, and adversely
Performance Assessment:  
impacted the cornerstone objective to provide reasonable assurance that physical design
barriers (fuel cladding, reactor coolant system, and containment) protect the public from
Performance Deficiency: The licensees failure on two occasions to identify a broken  
radionuclide releases caused by accidents or events. Specifically, the unaddressed condition
chemistry probe in the feedwater system had the potential to cause an adverse impact on  
of the broken probe remaining in the feedwater system resulted in damage to the feedwater
plant safety and to promptly implement appropriate measures to address that condition was a  
sparger, which resulted in thermal stresses to the reactor pressure vessel due to feedwater
performance deficiency.  
impingement on the inner reactor pressure vessel wall, as well as the introduction of foreign
material inside the reactor vessel having the potential to result in damaged fuel. The licensee
Screening: The inspectors determined the performance deficiency was more than minor  
performed an evaluation to determine what plant operational limitations were necessary in
because it was associated with the Cladding Performance, as well as the RCS Equipment  
order to ensure that additional thermal stresses on the reactor pressure vessel inner wall
and Barrier Performance, attributes of the Barrier Integrity Cornerstone, and adversely  
remained below a threshold that would challenge the structural integrity of the vessel.
impacted the cornerstone objective to provide reasonable assurance that physical design  
Significance: In accordance with Inspection Manual Chapter 0609, Appendix A, Section 5.0,
barriers (fuel cladding, reactor coolant system, and containment) protect the public from  
RCS boundary issues other than pressurized thermal shock are evaluated under the Initiating
radionuclide releases caused by accidents or events. Specifically, the unaddressed condition  
Events Cornerstone. Using Inspection Manual Chapter 0609, Appendix A, The Significance
of the broken probe remaining in the feedwater system resulted in damage to the feedwater  
Determination Process for Findings At-Power, Exhibit 1, Initiating Events Screening
sparger, which resulted in thermal stresses to the reactor pressure vessel due to feedwater  
Questions, the finding was screened, as a potential loss of coolant accident (LOCA) initiator,
impingement on the inner reactor pressure vessel wall, as well as the introduction of foreign  
as having very low safety significance (Green) because, after a reasonable assessment of
material inside the reactor vessel having the potential to result in damaged fuel. The licensee  
                                                  7
performed an evaluation to determine what plant operational limitations were necessary in  
order to ensure that additional thermal stresses on the reactor pressure vessel inner wall  
remained below a threshold that would challenge the structural integrity of the vessel.  
Significance: In accordance with Inspection Manual Chapter 0609, Appendix A, Section 5.0,  
RCS boundary issues other than pressurized thermal shock are evaluated under the Initiating  
Events Cornerstone. Using Inspection Manual Chapter 0609, Appendix A, The Significance  
Determination Process for Findings At-Power, Exhibit 1, Initiating Events Screening  
Questions, the finding was screened, as a potential loss of coolant accident (LOCA) initiator,  
as having very low safety significance (Green) because, after a reasonable assessment of  


degradation, the finding could not result in exceeding the RCS leak rate for a small LOCA and
could not have likely affected other systems used to mitigate a LOCA.
Cross-cutting Aspect: A cross-cutting aspect of P.5, Operating Experience, was determined
8
to be applicable to the performance deficiencies; however, no cross-cutting aspect was
assigned since the performance deficiencies occurred in 2004 and 2011, and are not
degradation, the finding could not result in exceeding the RCS leak rate for a small LOCA and  
indicative of current licensee performance.
could not have likely affected other systems used to mitigate a LOCA.  
Enforcement:
Violation: Title 10 CFR Part 50, Appendix B, Criterion XVI, requires, in part, that measures
Cross-cutting Aspect: A cross-cutting aspect of P.5, Operating Experience, was determined  
shall be established to assure that conditions adverse to quality, such as failures,
to be applicable to the performance deficiencies; however, no cross-cutting aspect was  
malfunctions, deficiencies, deviations, defective material and equipment, and
assigned since the performance deficiencies occurred in 2004 and 2011, and are not  
nonconformances are promptly identified and corrected. Contrary to the above, from
indicative of current licensee performance.  
June 2004 to January 2018, the licensee failed to establish measures to assure that a
Enforcement:  
condition adverse to quality was promptly identified and corrected. Specifically, the licensee
failed to identify and correct a condition involving a broken sampling probe inside the
Violation: Title 10 CFR Part 50, Appendix B, Criterion XVI, requires, in part, that measures  
feedwater system. The uncorrected condition resulted in damage to a feedwater sparger,
shall be established to assure that conditions adverse to quality, such as failures,  
with the potential to impact the available margin for integrity of the reactor vessel.
malfunctions, deficiencies, deviations, defective material and equipment, and  
Disposition: This violation is being treated as a non-cited violation, consistent with
nonconformances are promptly identified and corrected. Contrary to the above, from  
Section 2.3.2.a of the Enforcement Policy.
June 2004 to January 2018, the licensee failed to establish measures to assure that a  
Failure to Provide Adequate Procedures for Post-Scram Recovery
condition adverse to quality was promptly identified and corrected. Specifically, the licensee  
Cornerstone         Significance                                   Cross-cutting   Report
failed to identify and correct a condition involving a broken sampling probe inside the  
                                                                    Aspect          Section
feedwater system. The uncorrected condition resulted in damage to a feedwater sparger,  
Mitigating         Green                                           None            71111.18 -
with the potential to impact the available margin for integrity of the reactor vessel.  
Systems            NCV 05000458/2018012-06                                         Plant
                    Closed                                                          Modifications
Disposition: This violation is being treated as a non-cited violation, consistent with  
The inspectors reviewed a self-revealing, non-cited violation of Technical Specification 5.4.1.a
Section 2.3.2.a of the Enforcement Policy.  
for the licensees failure to establish, implement and maintain a procedure required by
Regulatory Guide 1.33, Revision 2, Appendix A, dated February 1978. Specifically,
Failure to Provide Adequate Procedures for Post-Scram Recovery  
Procedure OSP-0053, Emergency and Transient Response Support Procedure,
Cornerstone  
Revision 22, which is required by Regulatory Guide 1.33, inappropriately directed operations
Significance  
personnel to establish feedwater flow to the reactor pressure vessel using the main feedwater
Cross-cutting  
regulating valve (MFRV) as part of the post-scram actions. This resulted in the MFRVs being
Aspect
operated outside their design limits. This resulted in catastrophic failure of the MFRV
Report  
variseals and subsequent damage to multiple fuel assemblies.
Section  
Description:
Mitigating  
In January 2015, the licensee revised Procedure OSP-0053, Emergency And Transient
Systems
Response Support Procedure, to use one of the three MFRVs to control reactor water level
Green  
following a scram event, and not use C33-LVF002, Start-Up FRV, which is designed to be
NCV 05000458/2018012-06  
used for this application. This resulted in proceduralizing the use of a MFRV in circumstances
Closed
below the minimum controllable flow for the MFRV of 209,000 lbs/hr that the Main FRV
None
Copes Vulcan sizing datasheet provides as the a minimum controllable flow condition. As a
71111.18 -
result of this change to the procedure to use a MFRV, the valves cycled numerous times in
Plant  
the process of controlling level at low flow post-scram when feedwater flow demand was
Modifications  
below the MFRV minimum controllable flow volume. This repeated cycling of the valve led to
The inspectors reviewed a self-revealing, non-cited violation of Technical Specification 5.4.1.a  
excessive open/close cycling of the MFRVs and caused the catastrophic failure of the
for the licensees failure to establish, implement and maintain a procedure required by  
variseals.
Regulatory Guide 1.33, Revision 2, Appendix A, dated February 1978. Specifically,  
                                                  8
Procedure OSP-0053, Emergency and Transient Response Support Procedure,  
Revision 22, which is required by Regulatory Guide 1.33, inappropriately directed operations  
personnel to establish feedwater flow to the reactor pressure vessel using the main feedwater  
regulating valve (MFRV) as part of the post-scram actions. This resulted in the MFRVs being  
operated outside their design limits. This resulted in catastrophic failure of the MFRV  
variseals and subsequent damage to multiple fuel assemblies.  
Description:  
In January 2015, the licensee revised Procedure OSP-0053, Emergency And Transient  
Response Support Procedure, to use one of the three MFRVs to control reactor water level  
following a scram event, and not use C33-LVF002, Start-Up FRV, which is designed to be  
used for this application. This resulted in proceduralizing the use of a MFRV in circumstances  
below the minimum controllable flow for the MFRV of 209,000 lbs/hr that the Main FRV  
Copes Vulcan sizing datasheet provides as the a minimum controllable flow condition. As a  
result of this change to the procedure to use a MFRV, the valves cycled numerous times in  
the process of controlling level at low flow post-scram when feedwater flow demand was  
below the MFRV minimum controllable flow volume. This repeated cycling of the valve led to  
excessive open/close cycling of the MFRVs and caused the catastrophic failure of the  
variseals.  


As a result, foreign material parts of the variseal were introduced into the core. It is
suspected that this material resulted in six nuclear fuel cladding failures caused by debris
fretting.
9
Corrective Actions: The licensee revised Procedure OSP-0053, Emergency and Transient
Response Support Procedure, to control reactor vessel level post scram using a startup
As a result, foreign material parts of the variseal were introduced into the core. It is  
feedwater regulating valve and modified the design of the MFRV variseal.
suspected that this material resulted in six nuclear fuel cladding failures caused by debris  
Corrective Action Reference: CR-RBS-2016-00893
fretting.  
Performance Assessment:
Performance Deficiency: The failure to establish adequate procedural guidance for operation
Corrective Actions: The licensee revised Procedure OSP-0053, Emergency and Transient  
of the main feedwater system was a performance deficiency.
Response Support Procedure, to control reactor vessel level post scram using a startup  
Screening: The performance deficiency was more than minor, and therefore a finding,
feedwater regulating valve and modified the design of the MFRV variseal.  
because it was associated with the procedure quality attribute of the Mitigating Systems
Cornerstone and adversely affected the cornerstone objective to ensure the availability,
Corrective Action Reference: CR-RBS-2016-00893  
reliability, and capability of systems that respond to initiating events to prevent undesirable
Performance Assessment:  
consequences. Specifically, Procedure OSP-0053, Emergency and Transient Response
Support Procedure, Revision 22, inappropriately directed operations personnel to establish
Performance Deficiency: The failure to establish adequate procedural guidance for operation  
feedwater flow to the reactor pressure vessel using the MFRV as part of the post-scram
of the main feedwater system was a performance deficiency.  
actions. This resulted in the MFRVs being operated outside their design limits.
Significance: The inspectors screened the finding in accordance with Inspection Manual
Screening: The performance deficiency was more than minor, and therefore a finding,  
Chapter 0609, Appendix A, The Significance Determination Process for (SDP) for Findings
because it was associated with the procedure quality attribute of the Mitigating Systems  
At-Power. Using Inspection Manual Chapter 0609, Appendix A, Exhibit 2, Mitigating
Cornerstone and adversely affected the cornerstone objective to ensure the availability,  
Systems Screening Questions, the inspectors determined this finding was of very low safety
reliability, and capability of systems that respond to initiating events to prevent undesirable  
significance (Green) because the finding: (1) was not a deficiency affecting the design or
consequences. Specifically, Procedure OSP-0053, Emergency and Transient Response  
qualification of a mitigating structure, system, or component, and did not result in a loss of
Support Procedure, Revision 22, inappropriately directed operations personnel to establish  
operability or functionality; (2) did not represent a loss of system and/or function; (3) did not
feedwater flow to the reactor pressure vessel using the MFRV as part of the post-scram  
represent an actual loss of function of at least a single train for longer than its technical
actions. This resulted in the MFRVs being operated outside their design limits.  
specification allowed outage time, or two separate safety systems out-of-service for longer
than their technical specification allowed outage time; and (4) did not represent an actual loss
Significance: The inspectors screened the finding in accordance with Inspection Manual  
of function of one or more nontechnical specification trains of equipment designated as high
Chapter 0609, Appendix A, The Significance Determination Process for (SDP) for Findings  
safety-significant in accordance with the licensees maintenance rule program.
At-Power. Using Inspection Manual Chapter 0609, Appendix A, Exhibit 2, Mitigating  
Cross-cutting Aspect: No cross-cutting aspect was assigned since the performance
Systems Screening Questions, the inspectors determined this finding was of very low safety  
deficiency occurred in January 2015 and is not indicative of current licensee performance.
significance (Green) because the finding: (1) was not a deficiency affecting the design or  
Enforcement:
qualification of a mitigating structure, system, or component, and did not result in a loss of  
Violation: Technical Specification 5.4.1.a requires in part, that written procedures shall be
operability or functionality; (2) did not represent a loss of system and/or function; (3) did not  
established, implemented, and maintained covering the applicable procedures recommended
represent an actual loss of function of at least a single train for longer than its technical  
in Regulatory Guide 1.33, Revision 2, Appendix A, dated February 1978. Regulatory
specification allowed outage time, or two separate safety systems out-of-service for longer  
Guide 1.33, Appendix A, Section 6.u., identifies procedures for responding to a reactor trip as
than their technical specification allowed outage time; and (4) did not represent an actual loss  
required procedures. Procedure OSP-0053, Attachment 16, Post Scram
of function of one or more nontechnical specification trains of equipment designated as high  
Feedwater/Condensate Manipulations Below 5% Reactor Power, was a procedure
safety-significant in accordance with the licensees maintenance rule program.
established by the licensee for responding to a reactor trip.
Contrary to the above, from January 30, 2015, until April 13, 2017, the licensee failed to
Cross-cutting Aspect: No cross-cutting aspect was assigned since the performance  
maintain adequate written procedures for responding to a reactor trip. Specifically,
deficiency occurred in January 2015 and is not indicative of current licensee performance.  
Procedure OSP-0053 inappropriately directed operations personnel to establish feedwater
Enforcement:  
                                                  9
Violation: Technical Specification 5.4.1.a requires in part, that written procedures shall be  
established, implemented, and maintained covering the applicable procedures recommended  
in Regulatory Guide 1.33, Revision 2, Appendix A, dated February 1978. Regulatory  
Guide 1.33, Appendix A, Section 6.u., identifies procedures for responding to a reactor trip as  
required procedures. Procedure OSP-0053, Attachment 16, Post Scram  
Feedwater/Condensate Manipulations Below 5% Reactor Power, was a procedure  
established by the licensee for responding to a reactor trip.  
Contrary to the above, from January 30, 2015, until April 13, 2017, the licensee failed to  
maintain adequate written procedures for responding to a reactor trip. Specifically,  
Procedure OSP-0053 inappropriately directed operations personnel to establish feedwater  


flow to the reactor pressure vessel using the MFRV as part of the post-scram actions. The
MFRV operator characteristics are not designed to operate at the low flow conditions
immediately following a reactor scram from high power. As a result, the MFRV variseals
10
degraded and resulted in damage to multiple fuel assemblies. Subsequent to the event, the
licensee changed the procedure, directing operations personnel to utilize one of the startup
flow to the reactor pressure vessel using the MFRV as part of the post-scram actions. The  
feedwater regulating valves.
MFRV operator characteristics are not designed to operate at the low flow conditions  
Disposition: This violation is being treated as an non-cited violation consistent with
immediately following a reactor scram from high power. As a result, the MFRV variseals  
Section 2.3.2.a of the NRC Enforcement Policy.
degraded and resulted in damage to multiple fuel assemblies. Subsequent to the event, the  
Failure to Develop an Adequate Operational Decision-Making Issue for Compensatory
licensee changed the procedure, directing operations personnel to utilize one of the startup  
Measures Related to a Degraded Condition of the Feedwater System Sparger Nozzles
feedwater regulating valves.  
Cornerstone       Significance                                 Cross-cutting Report Section
                                                                Aspect
Disposition: This violation is being treated as an non-cited violation consistent with  
Mitigating        Green                                         [H.9] -           71111.15 -
Section 2.3.2.a of the NRC Enforcement Policy.  
Systems            NCV 05000458/2018012-05                      Human            Operability
                  Closed                                        Performance, Determinations
Failure to Develop an Adequate Operational Decision-Making Issue for Compensatory  
                                                                Training          and
Measures Related to a Degraded Condition of the Feedwater System Sparger Nozzles  
                                                                                  Functionality
Cornerstone  
                                                                                  Assessments
Significance  
The inspectors identified a Green non-cited violation of 10 CFR Part 50, Appendix B,
Cross-cutting  
Criterion V, Instructions, Procedures, and Drawings, for the failure to develop an adequate
Aspect
operational decision-making issue (ODMI) document per Procedure EN-OP-111, Operational
Report Section  
Decision-Making Issue Process. Specifically, the licensee failed to develop an ODMI that
Mitigating
provided adequate guidance to the operators for safely operating the plant with degraded
Systems
feedwater sparger nozzles.
Green  
Description:
NCV 05000458/2018012-05
During a reactor startup on February 1, 2018, reactor recirculation pump B unexpectedly
Closed
tripped during an attempted upshift to fast speed. As a result, the plant was operating with
[H.9] -  
recirculation pump A in fast speed and recirculation pump B not running. Prior to this startup,
Human
during an outage that was being conducted to replace failed fuel assemblies, damage to
Performance,
feedwater sparger nozzles was identified.
Training
Example 1: The evaluation of the damaged feedwater sparger nozzles 7 and 8 on
71111.15 -
sparger N4C identified that the damaged sections of the feedwater sparger nozzles had the
Operability  
potential to adversely affect the vessel cladding by allowing relatively colder water to directly
Determinations  
flow into the relatively hotter vessel wall, thus inducing thermal fatigue. All components of the
and  
reactor coolant system (RCS) are designed to withstand effects of cyclic loads due to system
Functionality  
pressure and temperature changes. These loads are introduced by startup (heatup) and
Assessments  
shutdown (cooldown) operations, power transients, and reactor trips. Limits are established
The inspectors identified a Green non-cited violation of 10 CFR Part 50, Appendix B,  
for pressure and temperature changes during RCS heatup and cooldown, such that plant
Criterion V, Instructions, Procedures, and Drawings, for the failure to develop an adequate  
systems remain within the design assumptions and the stress limits for cyclic operation.
operational decision-making issue (ODMI) document per Procedure EN-OP-111, Operational  
Limits on RCS pressure, temperature, heatup rate, and cooldown rate define allowable
Decision-Making Issue Process. Specifically, the licensee failed to develop an ODMI that  
operating regions and operating cycles to prevent nonductile failure of system components.
provided adequate guidance to the operators for safely operating the plant with degraded  
Because operation with the sparger nozzle damage was outside the limits originally analyzed,
feedwater sparger nozzles.  
the licensee requested General Electric-Hitachi (GEH) to provide an operability analysis of
Description:  
the degraded condition. GEH Report 004N6557, Revision 0, dated January 26, 2018,
Operability Assessment of the River Bend Station Feedwater Sparger Assembly in the
During a reactor startup on February 1, 2018, reactor recirculation pump B unexpectedly  
January 2018 As-found Condition, stated, in part, this evaluation does not account for Final
tripped during an attempted upshift to fast speed. As a result, the plant was operating with  
                                                  10
recirculation pump A in fast speed and recirculation pump B not running. Prior to this startup,  
during an outage that was being conducted to replace failed fuel assemblies, damage to  
feedwater sparger nozzles was identified.  
Example 1: The evaluation of the damaged feedwater sparger nozzles 7 and 8 on  
sparger N4C identified that the damaged sections of the feedwater sparger nozzles had the  
potential to adversely affect the vessel cladding by allowing relatively colder water to directly  
flow into the relatively hotter vessel wall, thus inducing thermal fatigue. All components of the  
reactor coolant system (RCS) are designed to withstand effects of cyclic loads due to system  
pressure and temperature changes. These loads are introduced by startup (heatup) and  
shutdown (cooldown) operations, power transients, and reactor trips. Limits are established  
for pressure and temperature changes during RCS heatup and cooldown, such that plant  
systems remain within the design assumptions and the stress limits for cyclic operation.
Limits on RCS pressure, temperature, heatup rate, and cooldown rate define allowable  
operating regions and operating cycles to prevent nonductile failure of system components.
Because operation with the sparger nozzle damage was outside the limits originally analyzed,  
the licensee requested General Electric-Hitachi (GEH) to provide an operability analysis of  
the degraded condition. GEH Report 004N6557, Revision 0, dated January 26, 2018,  
Operability Assessment of the River Bend Station Feedwater Sparger Assembly in the  
January 2018 As-found Condition, stated, in part, this evaluation does not account for Final  


Feedwater Temperature Reduction (FFWTR), Feedwater Heater Out-of-Service (FWH OOS)
conditions, nor Single Loop Operation (SLO) operating conditions. Based on this analysis,
the licensees engineering department concluded that the recommended classification of this
11
condition was OPERABLE-COMP MEAS (operable with compensatory measures), with the
degraded/nonconforming condition being the holes in the feedwater sparger nozzles. Based
Feedwater Temperature Reduction (FFWTR), Feedwater Heater Out-of-Service (FWH OOS)  
on the results of this analysis, one of the operational restrictions/limitations stipulated in the
conditions, nor Single Loop Operation (SLO) operating conditions. Based on this analysis,  
licensees ODMI was that, RBS will not operate in Single Loop Operation (SLO).
the licensees engineering department concluded that the recommended classification of this  
The ODMI developed by the licensee included two trigger points:
condition was OPERABLE-COMP MEAS (operable with compensatory measures), with the  
Trigger Point 1:
degraded/nonconforming condition being the holes in the feedwater sparger nozzles. Based  
An unexpected operational state below approximately 85 percent power in which the vessel
on the results of this analysis, one of the operational restrictions/limitations stipulated in the  
wall-to-feedwater delta-T stabilizes at less than or equal to 154 degrees Fahrenheit (F), as
licensees ODMI was that, RBS will not operate in Single Loop Operation (SLO).  
detected by periodic monitoring during normal operations, OR due to a transient as defined
above.
The ODMI developed by the licensee included two trigger points:  
Trigger Point 2:
An unexpected operational state in which the vessel wall-to-feedwater delta-T stabilizes at
Trigger Point 1:  
greater than 154 degrees F, as detected by periodic monitoring during normal operations, OR
due to a transient as defined above.
An unexpected operational state below approximately 85 percent power in which the vessel  
The ODMI failed to provide adequate guidance to the operators if they found themselves in
wall-to-feedwater delta-T stabilizes at less than or equal to 154 degrees Fahrenheit (F), as  
any of the conditions that GEH had listed as not being evaluated for continued operation with
detected by periodic monitoring during normal operations, OR due to a transient as defined  
the degraded condition. When reactor recirculation pump B failed to shift to fast speed at
above.  
9:46 a.m., the operators logged entry into Procedure GOP-004, Single Loop Operations.
The plant was in single loop operating conditions, and remained there until 10:57 a.m. when
Trigger Point 2:  
the Mode switch was placed in shutdown. The ODMI failed to provide adequate guidance on
the actions required if the plant entered any of the conditions that were not evaluated for the
An unexpected operational state in which the vessel wall-to-feedwater delta-T stabilizes at  
degraded sparger condition. In addition, the Just In Time Training given to the operators
greater than 154 degrees F, as detected by periodic monitoring during normal operations, OR  
prior to taking the watch to commence power operations with the degraded condition did not
due to a transient as defined above.  
address these issues either. As a result, rather than take prompt actions to place the plant in
a known safe condition upon entry into single loop operations, the control room supervisor
The ODMI failed to provide adequate guidance to the operators if they found themselves in  
requested that GEH be contacted to determine if it was acceptable to remain in single loop
any of the conditions that GEH had listed as not being evaluated for continued operation with  
operations.
the degraded condition. When reactor recirculation pump B failed to shift to fast speed at  
Example 2: The evaluation of the damaged feedwater sparger nozzles 7 and 8 on
9:46 a.m., the operators logged entry into Procedure GOP-004, Single Loop Operations.
sparger N4C identified that the damaged sections of the feedwater sparger nozzles had the
The plant was in single loop operating conditions, and remained there until 10:57 a.m. when  
potential to adversely affect the B narrow range level instrument. The damage on feedwater
the Mode switch was placed in shutdown. The ODMI failed to provide adequate guidance on  
sparger N4C created unexpected feedwater flow paths in the reactor vessel during plant
the actions required if the plant entered any of the conditions that were not evaluated for the  
operation that had the potential to adversely affect the "B" variable leg reactor water level
degraded sparger condition. In addition, the Just In Time Training given to the operators  
instruments. There were two potential impacts of this condition on indicated level from
prior to taking the watch to commence power operations with the degraded condition did not  
narrow range level instruments that tap off of the B variable leg. Flow from the holes in the
address these issues either. As a result, rather than take prompt actions to place the plant in  
feedwater sparger nozzle elbows could flow across the variable leg nozzle opening at AZ
a known safe condition upon entry into single loop operations, the control room supervisor  
200 degrees (B Leg), lowering the pressure on the variable leg side of the differential
requested that GEH be contacted to determine if it was acceptable to remain in single loop  
pressure measurements, or the flow from the sparger nozzle damage could directly impact
operations.  
the B variable leg, increasing the pressure on the variable leg side of the differential pressure
measurements.
Example 2: The evaluation of the damaged feedwater sparger nozzles 7 and 8 on  
                                                11
sparger N4C identified that the damaged sections of the feedwater sparger nozzles had the  
potential to adversely affect the B narrow range level instrument. The damage on feedwater  
sparger N4C created unexpected feedwater flow paths in the reactor vessel during plant  
operation that had the potential to adversely affect the "B" variable leg reactor water level  
instruments. There were two potential impacts of this condition on indicated level from  
narrow range level instruments that tap off of the B variable leg. Flow from the holes in the  
feedwater sparger nozzle elbows could flow across the variable leg nozzle opening at AZ  
200 degrees (B Leg), lowering the pressure on the variable leg side of the differential  
pressure measurements, or the flow from the sparger nozzle damage could directly impact  
the B variable leg, increasing the pressure on the variable leg side of the differential pressure  
measurements.  


The narrow range RPV level instrumentation supports two reactor water level trips: low level
(Level 3) and high level (Level 8). During a transient or accident event where the RPV water
level is changing, the trip signal from the B narrow range instrument could be affected.
12
Based on the GE report, during a transient or accident event where the RPV water level is
increasing, the high level (Level 8) trips (RPS trip and Feedwater Pump trip) in the affected
The narrow range RPV level instrumentation supports two reactor water level trips: low level  
channel may occur later than the trips in the unaffected channels. This may delay the overall
(Level 3) and high level (Level 8). During a transient or accident event where the RPV water  
Level 8 trips. For the Level 8 RPS trip, the margin between the calculated nominal trip
level is changing, the trip signal from the B narrow range instrument could be affected.  
setpoint and the technical specification allowable value is 0.77 inches. For the Level 3 RPS
trip, the margin between the calculated nominal trip setpoint and the technical specification
Based on the GE report, during a transient or accident event where the RPV water level is  
allowable value is 0.67 inches. An operability determination of the narrow range level
increasing, the high level (Level 8) trips (RPS trip and Feedwater Pump trip) in the affected  
instruments was performed under CR-RBS-2018-00633 CA-01.
channel may occur later than the trips in the unaffected channels. This may delay the overall  
The ODMI developed by the licensee included two trigger points:
Level 8 trips. For the Level 8 RPS trip, the margin between the calculated nominal trip  
Trigger Point 1:
setpoint and the technical specification allowable value is 0.77 inches. For the Level 3 RPS  
Action: Refer to applicable SRs as specified by STP-000-0001, Att. 9.2
trip, the margin between the calculated nominal trip setpoint and the technical specification  
      Step 30 in STP-000-0001 not within 4 inches
allowable value is 0.67 inches. An operability determination of the narrow range level  
      Step 71 in STP-000-0001 not within 6 inches
instruments was performed under CR-RBS-2018-00633 CA-01.
Notify the Duty Manager and the Ops Duty Manager
Trigger Point 2:
The ODMI developed by the licensee included two trigger points:  
The magnitude of the B channel deviation is  1.5 inches in either direction from the average
of the A, C and D channel average + 1.1 inches.
Trigger Point 1:      
Notify the Duty Manager and the Engineering Duty Manager.
Action: Refer to applicable SRs as specified by STP-000-0001, Att. 9.2
The ODMI implemented by the licensee allowed level indication deviation in the affected
      Step 30 in STP-000-0001 not within 4 inches  
channel for the B21-LTN080 instruments to be monitored to ensure it remained within the
      Step 71 in STP-000-0001 not within 6 inches  
allowable margin to ensure the technical specification trip limit is not exceeded. It stated in
Notify the Duty Manager and the Ops Duty Manager  
part that, If the deviation exceeds a change of 1.5 inches from historical deviation of
1.1 inches above the average of the A, C, and D channels in either an increasing or
Trigger Point 2:
decreasing direction, then condition will be evaluated by engineering. The monitored trigger
The magnitude of the B channel deviation is  1.5 inches in either direction from the average  
point of +1.5 inches will provide adequate margin for both the Level 3 and Level 8 trips.
of the A, C and D channel average + 1.1 inches.  
However, if a 1.5-inch bias in the low direction would have been reached, two Technical
Notify the Duty Manager and the Engineering Duty Manager.  
Specification (TS) Allowable Values could have been exceeded (by 0.5 inches for TS
Table 3.3.5.2-1, Function 2, Reactor Core Isolation Cooling System Instrumentation, and by
The ODMI implemented by the licensee allowed level indication deviation in the affected  
0.49 inches for TS Table 3.3.5.2-1, Function 5, Reactor Protection System Instrumentation).
channel for the B21-LTN080 instruments to be monitored to ensure it remained within the  
The 1.5-inch bias in the low direction would have rendered the instrument inoperable based
allowable margin to ensure the technical specification trip limit is not exceeded. It stated in  
on 10 CFR 50.36(c)(2)(i), which states, Limiting conditions for operation are the lowest
part that, If the deviation exceeds a change of 1.5 inches from historical deviation of  
functional capability or performance levels of equipment required for safe operation of the
1.1 inches above the average of the A, C, and D channels in either an increasing or  
facility. Since the limiting conditions for operations (LCOs) include Allowable Values (e.g.,
decreasing direction, then condition will be evaluated by engineering. The monitored trigger  
LCO 3.3.5.2 includes Table 3.3.5.2-1 which has Allowable Values for Functions 2 and 5), the
point of +1.5 inches will provide adequate margin for both the Level 3 and Level 8 trips.
Allowable Values are understood to be the lowest functional capability or performance levels
However, if a 1.5-inch bias in the low direction would have been reached, two Technical  
of equipment required for safe operation of the facility.
Specification (TS) Allowable Values could have been exceeded (by 0.5 inches for TS  
The licensees technical specifications provide the following guidance: Surveillance
Table 3.3.5.2-1, Function 2, Reactor Core Isolation Cooling System Instrumentation, and by  
Requirement 3.0.1, Failure to meet a Surveillance, whether such failure is experienced
0.49 inches for TS Table 3.3.5.2-1, Function 5, Reactor Protection System Instrumentation).
during the performance of the Surveillance or between performances of the Surveillance,
The 1.5-inch bias in the low direction would have rendered the instrument inoperable based  
shall be failure to meet the LCO.
on 10 CFR 50.36(c)(2)(i), which states, Limiting conditions for operation are the lowest  
                                                12
functional capability or performance levels of equipment required for safe operation of the  
facility. Since the limiting conditions for operations (LCOs) include Allowable Values (e.g.,  
LCO 3.3.5.2 includes Table 3.3.5.2-1 which has Allowable Values for Functions 2 and 5), the  
Allowable Values are understood to be the lowest functional capability or performance levels  
of equipment required for safe operation of the facility.  
The licensees technical specifications provide the following guidance: Surveillance  
Requirement 3.0.1, Failure to meet a Surveillance, whether such failure is experienced  
during the performance of the Surveillance or between performances of the Surveillance,  
shall be failure to meet the LCO.


1.1 Definitions: A CHANNEL CALIBRATION shall be the adjustment, as necessary, of the
channel output such that it responds within the necessary range and accuracy to known
values of the parameter that the channel monitors
13
In addition, the TS Bases state, SR 3.0.1 through SR 3.0.4 establish the general
requirements applicable to all Specifications and apply at all times, unless otherwise stated.
1.1 Definitions: A CHANNEL CALIBRATION shall be the adjustment, as necessary, of the  
The OPERABILITY of the RPS (Reactor Protection System) is dependent on the
channel output such that it responds within the necessary range and accuracy to known  
OPERABILITY of the individual instrumentation channel Functions specified in
values of the parameter that the channel monitors  
Table 3.3.1.1-1. Each Function must have a required number of OPERABLE channels [2 per
RPS trip system for the vessel level function] per RPS trip system, with their setpoints within
In addition, the TS Bases state, SR 3.0.1 through SR 3.0.4 establish the general  
the specified Allowable Value, where appropriate. The actual setpoint is calibrated consistent
requirements applicable to all Specifications and apply at all times, unless otherwise stated.
with applicable setpoint methodology assumptions. Each channel must also respond within
The OPERABILITY of the RPS (Reactor Protection System) is dependent on the  
its assumed response time. Allowable Values are specified for each RPS Function specified
OPERABILITY of the individual instrumentation channel Functions specified in  
in the Table. Nominal trip setpoints are specified in the setpoint calculations. The nominal
Table 3.3.1.1-1. Each Function must have a required number of OPERABLE channels [2 per  
setpoints are selected to ensure that the actual setpoints do not exceed the Allowable Value
RPS trip system for the vessel level function] per RPS trip system, with their setpoints within  
between successive channel calibrations. Operation with a trip setpoint less conservative
the specified Allowable Value, where appropriate. The actual setpoint is calibrated consistent  
than the nominal trip setpoint, but within its Allowable Value, is acceptable. A channel is
with applicable setpoint methodology assumptions. Each channel must also respond within  
inoperable if its actual trip setpoint is not within its required Allowable Value.
its assumed response time. Allowable Values are specified for each RPS Function specified  
Process effects impact the establishment of the appropriate Nominal Trip Setpoint, which is
in the Table. Nominal trip setpoints are specified in the setpoint calculations. The nominal  
determined by addressing all instrument channel uncertainties (including biases) and
setpoints are selected to ensure that the actual setpoints do not exceed the Allowable Value  
offsetting them from the Analytical Limit. The currently licensed Allowable Values are fixed
between successive channel calibrations. Operation with a trip setpoint less conservative  
within the technical specification tables. Nominal Trip Setpoints are established on the basis
than the nominal trip setpoint, but within its Allowable Value, is acceptable. A channel is  
of a calculation that identifies all known uncertainties between the Analytical Limit and the
inoperable if its actual trip setpoint is not within its required Allowable Value.
Nominal Trip Setpoint. If a new, unaccounted-for process effect bias in the nonconservative
direction is discovered, this effect needs to be reflected in the calculation of a new Nominal
Process effects impact the establishment of the appropriate Nominal Trip Setpoint, which is  
Trip Setpoint and a corresponding new Allowable Value. However, in this case, the licensee
determined by addressing all instrument channel uncertainties (including biases) and  
did not elect to pursue a license amendment or other process to change its currently licensed
offsetting them from the Analytical Limit. The currently licensed Allowable Values are fixed  
Allowable Value, nor did it ask for a temporary enforcement discretion. Therefore, with the
within the technical specification tables. Nominal Trip Setpoints are established on the basis  
new (unaccounted for) postulated process effect present, this has the effect of making the
of a calculation that identifies all known uncertainties between the Analytical Limit and the  
existing Nominal Trip Setpoint (calibrated value) offset in the nonconservative direction by the
Nominal Trip Setpoint. If a new, unaccounted-for process effect bias in the nonconservative  
amount of the new postulated process effect (i.e., up to 1.5 inches), which reduces the margin
direction is discovered, this effect needs to be reflected in the calculation of a new Nominal  
between the actual trip setpoint and the existing licensed Allowable Value.
Trip Setpoint and a corresponding new Allowable Value. However, in this case, the licensee  
Therefore, to meet the River Bend technical specification requirement that a channel be
did not elect to pursue a license amendment or other process to change its currently licensed  
considered inoperable if its actual trip setpoint is not within its required Allowable Value
Allowable Value, nor did it ask for a temporary enforcement discretion. Therefore, with the  
without changing the currently licensed Allowable Value, only approximately a 1/2-inch of the
new (unaccounted for) postulated process effect present, this has the effect of making the  
1.5 inches of new postulated process effect can be accommodated between the existing
existing Nominal Trip Setpoint (calibrated value) offset in the nonconservative direction by the  
calibrated setpoint and the (existing) licensed Allowable Value. Thus, the direction to notify
amount of the new postulated process effect (i.e., up to 1.5 inches), which reduces the margin  
engineering only if the Rx vessel level indication bias had reached a value of 1.5 inches in
between the actual trip setpoint and the existing licensed Allowable Value.  
either direction was inadequate direction for the operating staff in order to ensure that the
instruments remained operable.
Therefore, to meet the River Bend technical specification requirement that a channel be  
Corrective Actions: The licensee corrected the condition by revising the ODMI to include
considered inoperable if its actual trip setpoint is not within its required Allowable Value  
adequate operator guidance and trigger points.
without changing the currently licensed Allowable Value, only approximately a 1/2-inch of the  
Corrective Action Reference: CR-RBS-2018-03148
1.5 inches of new postulated process effect can be accommodated between the existing  
                                                  13
calibrated setpoint and the (existing) licensed Allowable Value. Thus, the direction to notify  
engineering only if the Rx vessel level indication bias had reached a value of 1.5 inches in  
either direction was inadequate direction for the operating staff in order to ensure that the  
instruments remained operable.  
Corrective Actions: The licensee corrected the condition by revising the ODMI to include  
adequate operator guidance and trigger points.  
Corrective Action Reference: CR-RBS-2018-03148  


Performance Assessment:
Performance Deficiency: The failure to establish ODMI guidance per Procedure EN-OP-111
to address the compensatory measures implemented to maintain operability of the plant with
14
degraded feedwater sparger nozzles was a performance deficiency.
Screening: For Example 1, the performance deficiency was more than minor, and therefore a
Performance Assessment:  
finding, because it was associated with the equipment reliability attribute of the Mitigating
Systems Cornerstone and adversely affected the cornerstone objective to ensure the
Performance Deficiency: The failure to establish ODMI guidance per Procedure EN-OP-111  
availability, reliability, and capability of systems that respond to initiating events to prevent
to address the compensatory measures implemented to maintain operability of the plant with  
undesirable consequences. Specifically, the licensee failed to provide adequate guidance to
degraded feedwater sparger nozzles was a performance deficiency.  
the operators for actions required if the plant inadvertently entered any of the unanalyzed
conditions for continued operation with the degraded sparger. For Example 2, the
Screening: For Example 1, the performance deficiency was more than minor, and therefore a  
performance deficiency was more than minor, and therefore a finding, because if left
finding, because it was associated with the equipment reliability attribute of the Mitigating  
uncorrected it would have the potential to lead to a more significant safety concern.
Systems Cornerstone and adversely affected the cornerstone objective to ensure the  
Specifically, the use of less conservative calculated values than the Allowable Values stated
availability, reliability, and capability of systems that respond to initiating events to prevent  
in the facility TS as a basis for establishing a threshold for operability of TS equipment could
undesirable consequences. Specifically, the licensee failed to provide adequate guidance to  
result in the inappropriate evaluation of actual degraded conditions that impact the ability of
the operators for actions required if the plant inadvertently entered any of the unanalyzed  
components to perform their required safety functions.
conditions for continued operation with the degraded sparger. For Example 2, the  
Significance: The inspectors screened the finding in accordance with Inspection Manual
performance deficiency was more than minor, and therefore a finding, because if left  
Chapter 0609, Appendix A, The Significance Determination Process for (SDP) for Findings
uncorrected it would have the potential to lead to a more significant safety concern.
At-Power. Using Inspection Manual Chapter 0609, Appendix A, Exhibit 1, Initiating Events
Specifically, the use of less conservative calculated values than the Allowable Values stated  
Screening Questions, the inspectors determined this finding was of very low safety
in the facility TS as a basis for establishing a threshold for operability of TS equipment could  
significance (Green) because for Example 1, the finding would not result in exceeding the
result in the inappropriate evaluation of actual degraded conditions that impact the ability of  
RCS leak rate for a small LOCA and could not have likely affected other systems used to
components to perform their required safety functions.  
mitigate a LOCA. For Example 2, it was not a design/qualification deficiency, did not
represent a loss of system safety function, did not result in a loss of function of a single train
Significance: The inspectors screened the finding in accordance with Inspection Manual  
Chapter 0609, Appendix A, The Significance Determination Process for (SDP) for Findings  
At-Power. Using Inspection Manual Chapter 0609, Appendix A, Exhibit 1, Initiating Events  
Screening Questions, the inspectors determined this finding was of very low safety  
significance (Green) because for Example 1, the finding would not result in exceeding the  
RCS leak rate for a small LOCA and could not have likely affected other systems used to  
mitigate a LOCA. For Example 2, it was not a design/qualification deficiency, did not  
represent a loss of system safety function, did not result in a loss of function of a single train  
for greater than its TS-allowable outage time, did not result in a loss of function of nonsafety-
for greater than its TS-allowable outage time, did not result in a loss of function of nonsafety-
related risk-significant equipment and was not risk significant due to external events. In
related risk-significant equipment and was not risk significant due to external events. In  
addition, no actual deviation of the B narrow range level instrument was observed during
addition, no actual deviation of the B narrow range level instrument was observed during  
plant startup on February 9, 2018.
plant startup on February 9, 2018.  
Cross-cutting Aspect: This finding had a cross-cutting aspect of human performance, change
management H.3: Leaders use a systematic process for evaluating and implementing
Cross-cutting Aspect: This finding had a cross-cutting aspect of human performance, change  
change so that nuclear safety remains the overriding priority. Specifically, the licensee did
management H.3: Leaders use a systematic process for evaluating and implementing  
not use a systematic process to develop and verify the adequacy of the ODMIs associated
change so that nuclear safety remains the overriding priority. Specifically, the licensee did  
with the compensatory measures implemented for the degraded sparger.
not use a systematic process to develop and verify the adequacy of the ODMIs associated  
Enforcement:
with the compensatory measures implemented for the degraded sparger.  
Violation: Title 10 CFR Part 50, Appendix B, Criterion V, requires in part that, activities
Enforcement:  
affecting quality shall be prescribed by documented instructions, procedures, or drawings, of
a type appropriate to the circumstances. Licensee Procedure EN-OP-111, Operational
Violation: Title 10 CFR Part 50, Appendix B, Criterion V, requires in part that, activities  
Decision-Making Issue (ODMI) Process, Revision 16, an Appendix B quality-related
affecting quality shall be prescribed by documented instructions, procedures, or drawings, of  
procedure, provides instructions for developing guidance for plant operation with
a type appropriate to the circumstances. Licensee Procedure EN-OP-111, Operational  
compensatory measures in place to maintain plant system operable with degraded
Decision-Making Issue (ODMI) Process, Revision 16, an Appendix B quality-related  
conditions. Procedure EN-OP-111, step 5.2.4, states that Operational Decision-Making
procedure, provides instructions for developing guidance for plant operation with  
Considerations should ensure that a course of action is selected based upon a critical
compensatory measures in place to maintain plant system operable with degraded  
consideration of risks and potential consequences, as well as a thorough understanding of
conditions. Procedure EN-OP-111, step 5.2.4, states that Operational Decision-Making  
alternate solutions. The final decision should be a deliberate act, providing clear direction,
Considerations should ensure that a course of action is selected based upon a critical  
trigger points, contingencies, and abort criteria. The Action Plans should provide clear
consideration of risks and potential consequences, as well as a thorough understanding of  
                                                  14
alternate solutions. The final decision should be a deliberate act, providing clear direction,  
trigger points, contingencies, and abort criteria. The Action Plans should provide clear  


guidance in each ODMI which delineate actions to be taken when conditions escalate
unexpectedly, conditions are outside the scope of the ODMI analysis, or actions are not able
to be implemented. Actions that contain recommendations to "consider or evaluate" in
15
response to triggers should be avoided. When such actions are used, a definite period to
finish the evaluation or consideration should be provided.
guidance in each ODMI which delineate actions to be taken when conditions escalate  
Contrary to the above, prior to February 1, 2018, the licensee failed to ensure that the ODMIs
unexpectedly, conditions are outside the scope of the ODMI analysis, or actions are not able  
provided a course of action based upon a critical consideration of risks and potential
to be implemented. Actions that contain recommendations to "consider or evaluate" in  
consequences, as well as a thorough understanding of alternate solutions; and that the final
response to triggers should be avoided. When such actions are used, a definite period to  
decision was a deliberate act providing clear direction, trigger points, contingencies, and abort
finish the evaluation or consideration should be provided.  
criteria. Specifically, the licensee failed to develop adequate guidance for the operators to
maintain safe operation of the plant with compensatory measures in place for degraded
Contrary to the above, prior to February 1, 2018, the licensee failed to ensure that the ODMIs  
feedwater sparger nozzles. The action plans failed to provide clear guidance in each ODMI
provided a course of action based upon a critical consideration of risks and potential  
to delineate actions to be taken when conditions escalate unexpectedly; instead, the actions
consequences, as well as a thorough understanding of alternate solutions; and that the final  
specified directed the operators to consult with offsite contractors regarding the acceptability
decision was a deliberate act providing clear direction, trigger points, contingencies, and abort  
of allowing the plant to remain in operation with given conditions.
criteria. Specifically, the licensee failed to develop adequate guidance for the operators to  
Disposition: This violation is being treated as a non-cited violation, consistent with
maintain safe operation of the plant with compensatory measures in place for degraded  
Section 2.3.2.a of the NRC Enforcement Policy.
feedwater sparger nozzles. The action plans failed to provide clear guidance in each ODMI  
Failure to Establish Procedural Guidance for Determining Core Flow During Unanticipated
to delineate actions to be taken when conditions escalate unexpectedly; instead, the actions  
Single Loop Operations
specified directed the operators to consult with offsite contractors regarding the acceptability  
Cornerstone       Significance                                   Cross-cutting Report
of allowing the plant to remain in operation with given conditions.  
                                                                  Aspect          Section
Initiating         Green                                           [P.3] -         71153 -
Disposition: This violation is being treated as a non-cited violation, consistent with  
Events            NCV 05000458/2018012-03                        Problem          Follow-up of
Section 2.3.2.a of the NRC Enforcement Policy.  
                  Closed                                          Identification  Events and
                                                                  and              Notices of
Failure to Establish Procedural Guidance for Determining Core Flow During Unanticipated  
                                                                  Resolution,      Enforcement
Single Loop Operations  
                                                                  Resolution      Discretion
Cornerstone  
The inspectors reviewed a self-revealed, non-cited violation of 10 CFR Part 50, Appendix B,
Significance  
Criterion V, Instructions, Procedures and Drawings, for the licensees failure to establish
Cross-cutting  
appropriate instructions in the abnormal operating procedure for thermal hydraulic
Aspect
instabilities. Specifically, the procedural step for determining core flow when in single loop
Report  
operations at low power did not provide appropriate instructions to operators. As a result,
Section  
station personnel could not conclusively determine core flow and inserted a manual reactor
Initiating  
scram.
Events
Description:
Green  
On February 1, 2018, with the unit in Mode 1 at approximately 27 percent power, reactor
NCV 05000458/2018012-03
recirculation pump B unexpectedly tripped during an upshift in the speed of the pump. As a
Closed
result, the reactor was in a single loop configuration with the recirculation pump A running in
[P.3] -  
fast speed and the recirculation pump B not running. Operators entered Abnormal Operating
Problem
Procedure AOP-0024, Thermal Hydraulic Instability Controls, Revision 30, as a result of the
Identification
unplanned entry into single loop operations. Step 5.8 of this procedure directed operators to
and
determine core flow and enter the General Operating Procedure GOP-004, for single loop
Resolution,
operations. Step 5.8 also instructed operators to determine core flow using process computer
Resolution
point B33NA01V when in a configuration with one recirculation pump in fast speed and one
71153 -  
recirculation pump off. Control room operators observed the value of this data point as
Follow-up of  
13.9 Mlbm/hr. The operators concluded that this value was not valid since the indicated flow
Events and  
                                                  15
Notices of  
Enforcement  
Discretion  
The inspectors reviewed a self-revealed, non-cited violation of 10 CFR Part 50, Appendix B,  
Criterion V, Instructions, Procedures and Drawings, for the licensees failure to establish  
appropriate instructions in the abnormal operating procedure for thermal hydraulic  
instabilities. Specifically, the procedural step for determining core flow when in single loop  
operations at low power did not provide appropriate instructions to operators. As a result,  
station personnel could not conclusively determine core flow and inserted a manual reactor  
scram.  
Description:  
On February 1, 2018, with the unit in Mode 1 at approximately 27 percent power, reactor  
recirculation pump B unexpectedly tripped during an upshift in the speed of the pump. As a  
result, the reactor was in a single loop configuration with the recirculation pump A running in  
fast speed and the recirculation pump B not running. Operators entered Abnormal Operating  
Procedure AOP-0024, Thermal Hydraulic Instability Controls, Revision 30, as a result of the  
unplanned entry into single loop operations. Step 5.8 of this procedure directed operators to  
determine core flow and enter the General Operating Procedure GOP-004, for single loop  
operations. Step 5.8 also instructed operators to determine core flow using process computer  
point B33NA01V when in a configuration with one recirculation pump in fast speed and one  
recirculation pump off. Control room operators observed the value of this data point as  
13.9 Mlbm/hr. The operators concluded that this value was not valid since the indicated flow  


was much lower than expected with one recirculation pump running in fast speed. The
operators then observed a value of 27.3 Mlbm/hr core flow using the ERIS data point for
B33NA01V. This value appeared to be a valid number based on the single loop operation
16
power/flow map contained in AOP-0024, Attachment 2. Normal data points are displayed in
ERIS with a white text, but control room operators observed the ERIS data point displayed in
was much lower than expected with one recirculation pump running in fast speed. The  
a magenta color. Additionally, the word suspect appeared adjacent to the data point for
operators then observed a value of 27.3 Mlbm/hr core flow using the ERIS data point for  
core flow. Control room operators contacted information technology personnel and attempted
B33NA01V. This value appeared to be a valid number based on the single loop operation  
to understand the magenta color and suspect information associated with the core flow data
power/flow map contained in AOP-0024, Attachment 2. Normal data points are displayed in  
point. Concurrently, operators attempted to validate core flow using alternate means but
ERIS with a white text, but control room operators observed the ERIS data point displayed in  
were unsuccessful as the alternate indications did not provide accurate core flow readings at
a magenta color. Additionally, the word suspect appeared adjacent to the data point for  
low reactor power when in a single loop configuration. After approximately one hour spent
core flow. Control room operators contacted information technology personnel and attempted  
seeking to understand the unfamiliar indication associated with B33NA01V, control room
to understand the magenta color and suspect information associated with the core flow data  
operators conducted a brief and made the decision to shut down the unit due to the
point. Concurrently, operators attempted to validate core flow using alternate means but  
uncertainties associated with the core flow data point. Following plant shutdown and
were unsuccessful as the alternate indications did not provide accurate core flow readings at  
subsequent troubleshooting and investigation, licensee personnel concluded that the
low reactor power when in a single loop configuration. After approximately one hour spent  
magenta text and suspect note associated with ERIS B33NA01V was an expected system
seeking to understand the unfamiliar indication associated with B33NA01V, control room  
response. Below approximately 40 percent core flow, the plant process computer shifts the
operators conducted a brief and made the decision to shut down the unit due to the  
calculation method from the primary means of calculating core flow using the sum of jet pump
uncertainties associated with the core flow data point. Following plant shutdown and  
flows to an alternate process that uses core plate differential pressure. As a result of shifting
subsequent troubleshooting and investigation, licensee personnel concluded that the  
to the alternate calculation of core flow, data point ERIS B33NA01V was programmed to turn
magenta text and suspect note associated with ERIS B33NA01V was an expected system  
magenta in color and display suspect to alert operators that the method of calculating core
response. Below approximately 40 percent core flow, the plant process computer shifts the  
flow had changed.
calculation method from the primary means of calculating core flow using the sum of jet pump  
The inspectors reviewed Condition Report CR-RBS-2012-07759. This condition report was
flows to an alternate process that uses core plate differential pressure. As a result of shifting  
generated by operations department personnel on December 19, 2012, and identified that
to the alternate calculation of core flow, data point ERIS B33NA01V was programmed to turn  
ERIS point B33NA01V indicated suspect and was not available for use. The condition
magenta in color and display suspect to alert operators that the method of calculating core  
report also stated that this data point was needed for determining core flow when the plant
flow had changed.  
configuration consisted of one recirculation pump running in fast speed and another
The inspectors reviewed Condition Report CR-RBS-2012-07759. This condition report was  
recirculation pump was off. The inspectors confirmed that this condition report was generated
generated by operations department personnel on December 19, 2012, and identified that  
during a single loop plant configuration that was the result of an unanticipated reactor
ERIS point B33NA01V indicated suspect and was not available for use. The condition  
recirculation pump A trip on December 19, 2012. The condition report corrective actions
report also stated that this data point was needed for determining core flow when the plant  
explained the reason for the suspect reading of ERIS point B33NA01V. No corrective
configuration consisted of one recirculation pump running in fast speed and another  
actions were generated to address AOP-0024, which directs licensed operators to validate
recirculation pump was off. The inspectors confirmed that this condition report was generated  
core flow in single loop operations. Additionally, no corrective actions were generated to
during a single loop plant configuration that was the result of an unanticipated reactor  
validate plant simulator response to unanticipated single loop operations.
recirculation pump A trip on December 19, 2012. The condition report corrective actions  
Corrective Actions: After this information was disseminated to licensed operators, the
explained the reason for the suspect reading of ERIS point B33NA01V. No corrective  
licensee implemented procedural changes to AOP-0024 that provided amplifying information
actions were generated to address AOP-0024, which directs licensed operators to validate  
regarding B33NA01V validated core flow. Specifically, the licensee revised the procedure on
core flow in single loop operations. Additionally, no corrective actions were generated to  
February 7, 2018, in order to 1) direct operators to determine core flow using ERIS data point
validate plant simulator response to unanticipated single loop operations.  
B33NA01V during single loop operations when core flow is below 40 percent and 2) provide
clear guidance regarding expected system response of the process computer data points
Corrective Actions: After this information was disseminated to licensed operators, the  
during abnormal flow configurations.
licensee implemented procedural changes to AOP-0024 that provided amplifying information  
Corrective Action Reference: CR-RBS-2018-00776
regarding B33NA01V validated core flow. Specifically, the licensee revised the procedure on  
Performance Assessment:
February 7, 2018, in order to 1) direct operators to determine core flow using ERIS data point  
Performance Deficiency: The failure to establish appropriate guidance to determine core flow
B33NA01V during single loop operations when core flow is below 40 percent and 2) provide  
during single loop operations in quality-related abnormal operating procedure AOP-0024,
clear guidance regarding expected system response of the process computer data points  
Thermal Hydraulic Instability Controls, Revision 30, was a performance deficiency.
during abnormal flow configurations.  
                                                16
Corrective Action Reference: CR-RBS-2018-00776  
Performance Assessment:  
Performance Deficiency: The failure to establish appropriate guidance to determine core flow  
during single loop operations in quality-related abnormal operating procedure AOP-0024,  
Thermal Hydraulic Instability Controls, Revision 30, was a performance deficiency.  


Screening: The performance deficiency was more than minor, and therefore a finding,
because it was associated with the procedure quality attribute of the Initiating Events
Cornerstone and adversely affected the cornerstone objective to limit the likelihood of events
17
that upset plant stability. Specifically, the failure to understand core flow data indicated by
plant process computer point B33NA01V and ERIS data point B33NA01V resulted in
Screening: The performance deficiency was more than minor, and therefore a finding,  
confusion and the ultimate decision to insert a manual reactor scram.
because it was associated with the procedure quality attribute of the Initiating Events  
Significance: The inspectors screened the finding in accordance with Inspection Manual
Cornerstone and adversely affected the cornerstone objective to limit the likelihood of events  
Chapter 0609, Appendix A, The Significance Determination Process for (SDP) for Findings
that upset plant stability. Specifically, the failure to understand core flow data indicated by  
At-Power. Using Inspection Manual Chapter 0609, Appendix A, Exhibit 1, Initiating Events
plant process computer point B33NA01V and ERIS data point B33NA01V resulted in  
Screening Questions, the inspectors determined this finding is of very low safety significance
confusion and the ultimate decision to insert a manual reactor scram.  
(Green) because the finding did not cause a reactor trip and the loss of mitigation equipment
relied upon to transition the plant from the onset of the trip to a stable shutdown condition.
Significance: The inspectors screened the finding in accordance with Inspection Manual  
Cross-cutting Aspect: This finding has a cross-cutting aspect in the area of problem
Chapter 0609, Appendix A, The Significance Determination Process for (SDP) for Findings  
identification and resolution, resolution, because the licensee failed to take effective
At-Power. Using Inspection Manual Chapter 0609, Appendix A, Exhibit 1, Initiating Events  
corrective actions to address issues in a timely manner commensurate with their safety
Screening Questions, the inspectors determined this finding is of very low safety significance  
significance. Specifically, the station failed to implement procedure changes to AOP-0024
(Green) because the finding did not cause a reactor trip and the loss of mitigation equipment  
after discovering similar confusing indications associated with B33NA01V on
relied upon to transition the plant from the onset of the trip to a stable shutdown condition.  
December 19, 2012.
Enforcement:
Cross-cutting Aspect: This finding has a cross-cutting aspect in the area of problem  
Violation: Title 10 CFR Part 50, Appendix B, Criterion V, requires in part that, activities
identification and resolution, resolution, because the licensee failed to take effective  
affecting quality shall be prescribed by documented instructions, procedures, or drawings, of
corrective actions to address issues in a timely manner commensurate with their safety  
a type appropriate to the circumstances.
significance. Specifically, the station failed to implement procedure changes to AOP-0024  
Contrary to the above, prior to February 7, 2018, the licensee failed to provide a procedure of
after discovering similar confusing indications associated with B33NA01V on  
a type appropriate to the circumstances for an activity affecting quality. Specifically,
December 19, 2012.  
AOP-0024, Thermal Hydraulic Stability Controls, a quality-related procedure, was not
Enforcement:  
appropriate to the circumstances. AOP-0024 did not provide accurate and adequate
instruction to operators to determine core flow during single loop operations. The licensee
Violation: Title 10 CFR Part 50, Appendix B, Criterion V, requires in part that, activities  
restored compliance by revising AOP-0024 to include accurate and adequate guidance to
affecting quality shall be prescribed by documented instructions, procedures, or drawings, of  
determine core flow during unanticipated single loop operations.
a type appropriate to the circumstances.  
Disposition: This violation is being treated as an non-cited violation consistent with
Section 2.3.2.a of the NRC Enforcement Policy.
Contrary to the above, prior to February 7, 2018, the licensee failed to provide a procedure of  
Failure to Perform 10 CFR 50.59 Evaluation for Main Feedwater System Sparger Nozzle
a type appropriate to the circumstances for an activity affecting quality. Specifically,  
Damage
AOP-0024, Thermal Hydraulic Stability Controls, a quality-related procedure, was not  
Cornerstone       Significance                                     Cross-cutting Report
appropriate to the circumstances. AOP-0024 did not provide accurate and adequate  
                                                                    Aspect          Section
instruction to operators to determine core flow during single loop operations. The licensee  
None               SL-IV                                             None            71111.18 -
restored compliance by revising AOP-0024 to include accurate and adequate guidance to  
                  NCV 05000458/2018012-07                                           Plant
determine core flow during unanticipated single loop operations.  
                  Closed                                                            Modifications
The inspectors identified a Severity Level IV NCV of 10 CFR 50.59, Changes, Tests, and
Disposition: This violation is being treated as an non-cited violation consistent with  
Experiments, for the licensees failure to provide a written safety evaluation for the
Section 2.3.2.a of the NRC Enforcement Policy.  
determination that operation with compensatory measures for damaged feedwater sparger
nozzles did not require a license amendment pursuant to 10 CFR 50.90, Application for
Failure to Perform 10 CFR 50.59 Evaluation for Main Feedwater System Sparger Nozzle  
amendment of license, construction permit, or early site permit. Specifically, the licensee
Damage  
                                                  17
Cornerstone  
Significance  
Cross-cutting  
Aspect
Report  
Section  
None  
SL-IV  
NCV 05000458/2018012-07  
Closed
None
71111.18 -
Plant  
Modifications  
The inspectors identified a Severity Level IV NCV of 10 CFR 50.59, Changes, Tests, and  
Experiments, for the licensees failure to provide a written safety evaluation for the  
determination that operation with compensatory measures for damaged feedwater sparger  
nozzles did not require a license amendment pursuant to 10 CFR 50.90, Application for  
amendment of license, construction permit, or early site permit. Specifically, the licensee  


failed to recognize that compensatory measures prohibiting operation in single loop
conditions were technical specification changes, and as such required prior NRC approval.
Description:
18
During an outage that was conducted to replace failed fuel assemblies in January 2018,
damage to feedwater sparger nozzles was identified. The evaluation of the damaged
failed to recognize that compensatory measures prohibiting operation in single loop  
feedwater sparger nozzles #7 and #8 on sparger N4C identified that the damaged sections of
conditions were technical specification changes, and as such required prior NRC approval.  
the feedwater sparger nozzles had the potential to adversely affect the vessel cladding by
Description:  
allowing relatively colder water to directly flow into the relatively hotter vessel wall, thus
inducing thermal fatigue. All components of the RCS are designed to withstand effects of
During an outage that was conducted to replace failed fuel assemblies in January 2018,  
cyclic loads due to system pressure and temperature changes. These loads are introduced
damage to feedwater sparger nozzles was identified. The evaluation of the damaged  
by startup (heatup) and shutdown (cooldown) operations, power transients, and reactor trips.
feedwater sparger nozzles #7 and #8 on sparger N4C identified that the damaged sections of  
Limits are established for pressure and temperature changes during RCS heatup and
the feedwater sparger nozzles had the potential to adversely affect the vessel cladding by  
cooldown, such that plant systems remain within the design assumptions and the stress limits
allowing relatively colder water to directly flow into the relatively hotter vessel wall, thus  
for cyclic operation. Limits on RCS pressure, temperature, heatup rate, and cooldown rate
inducing thermal fatigue. All components of the RCS are designed to withstand effects of  
define allowable operating regions and operating cycles to prevent nonductile failure of
cyclic loads due to system pressure and temperature changes. These loads are introduced  
system components. Because operation with the sparger nozzle damage was outside the
by startup (heatup) and shutdown (cooldown) operations, power transients, and reactor trips.
limits originally analyzed, the licensee requested General Electric-Hitachi (GEH) to provide an
Limits are established for pressure and temperature changes during RCS heatup and  
operability analysis of the degraded condition. GEH Report #004N6557 Revision 0, dated
cooldown, such that plant systems remain within the design assumptions and the stress limits  
January 26, 2018, Operability Assessment of the River Bend Station Feedwater Sparger
for cyclic operation. Limits on RCS pressure, temperature, heatup rate, and cooldown rate  
Assembly in the January 2018 As-found Condition, stated in part, this evaluation does not
define allowable operating regions and operating cycles to prevent nonductile failure of  
system components. Because operation with the sparger nozzle damage was outside the  
limits originally analyzed, the licensee requested General Electric-Hitachi (GEH) to provide an  
operability analysis of the degraded condition. GEH Report #004N6557 Revision 0, dated  
January 26, 2018, Operability Assessment of the River Bend Station Feedwater Sparger  
Assembly in the January 2018 As-found Condition, stated in part, this evaluation does not  
account for Final Feedwater Temperature Reduction (FFWTR), Feedwater Heater Out-of-
account for Final Feedwater Temperature Reduction (FFWTR), Feedwater Heater Out-of-
Service (FWH OOS) conditions, nor Single Loop Operation (SLO) operating conditions.
Service (FWH OOS) conditions, nor Single Loop Operation (SLO) operating conditions.  
Based on this analysis, the licensees engineering department concluded that the
recommended classification of this condition was OPERABLE-COMP MEAS (operable with
Based on this analysis, the licensees engineering department concluded that the  
compensatory measures), with the degraded/nonconforming condition being the holes in the
recommended classification of this condition was OPERABLE-COMP MEAS (operable with  
feedwater sparger nozzles. One of the operational restrictions/limitations was that, RBS will
compensatory measures), with the degraded/nonconforming condition being the holes in the  
not operate in Single Loop Operation (SLO). These compensatory measures directly
feedwater sparger nozzles. One of the operational restrictions/limitations was that, RBS will  
affected Technical Specification (TS) 3.4.1, Recirculation Loops Operating. The TS limiting
not operate in Single Loop Operation (SLO). These compensatory measures directly  
condition for operation (LCO) B, One recirculation loop shall be in operation, which is
affected Technical Specification (TS) 3.4.1, Recirculation Loops Operating. The TS limiting  
applicable when operating in Modes 1 and 2, had the following limitations:
condition for operation (LCO) B, One recirculation loop shall be in operation, which is  
1.       THERMAL POWER  77.6% rated thermal power (RTP);
applicable when operating in Modes 1 and 2, had the following limitations:  
2.       Total core flow within limits;
3.       LCO 3.2.1,"AVERAGE PLANAR LINEAR HEAT GENERATION RATE (APLHGR),"
1.  
single loop operation limits specified in the Core Operating Limits Reports (COLR);
THERMAL POWER  77.6% rated thermal power (RTP);  
4.       LCO 3.2.2,"MINIMUM CRITICAL POWER RATIO (MCPR)," single loop operation
2.  
limits specified in the COLR; and
Total core flow within limits;  
5.       LCO 3.3.1.1, "Reactor Protection System (RPS) Instrumentation," Function 2.b
3.  
(Average Power Range Monitors Flow Biased Simulated Thermal Power- High), Allowable
LCO 3.2.1,"AVERAGE PLANAR LINEAR HEAT GENERATION RATE (APLHGR),"  
Value for single loop operation as specified in the COLR.
single loop operation limits specified in the Core Operating Limits Reports (COLR);
The licensees compensatory measures established a more restrictive LCO whereby Single
4.  
Loop Operations are limited by more restrictive criteria than those stated in the existing LCO.
LCO 3.2.2,"MINIMUM CRITICAL POWER RATIO (MCPR)," single loop operation  
Specifically, the licensees compensatory measures stated that the station would not operate
limits specified in the COLR; and
in Single Loop Operation.
5.  
NRC Administrative Letter 98-10: Dispositioning of Technical Specifications That Are
LCO 3.3.1.1, "Reactor Protection System (RPS) Instrumentation," Function 2.b  
Insufficient To Assure Plant Safety, dated December 29, 1988, provides the following
(Average Power Range Monitors Flow Biased Simulated Thermal Power- High), Allowable  
guidance:
Value for single loop operation as specified in the COLR.  
                                                18
The licensees compensatory measures established a more restrictive LCO whereby Single  
Loop Operations are limited by more restrictive criteria than those stated in the existing LCO.
Specifically, the licensees compensatory measures stated that the station would not operate  
in Single Loop Operation.  
NRC Administrative Letter 98-10: Dispositioning of Technical Specifications That Are  
Insufficient To Assure Plant Safety, dated December 29, 1988, provides the following  
guidance:  


Title 10 of the Code of Federal Regulations, Section 50.36, Technical Specifications
requires that each TS limiting condition for operation (LCO) specify, at a minimum, the lowest
functional capability or performance level of equipment required for the safe operation of the
19
facility.
IMC0326 states, in part: Additionally, if a compensatory measure involves a temporary facility
Title 10 of the Code of Federal Regulations, Section 50.36, Technical Specifications  
or procedure change, 10 CFR 50.59 should be applied to the temporary change with the
requires that each TS limiting condition for operation (LCO) specify, at a minimum, the lowest  
intent to determine whether the temporary change/compensatory measure itself (not the
functional capability or performance level of equipment required for the safe operation of the  
degraded or nonconforming condition) impacts other aspects of the facility or procedures
facility.  
described in the UFSAR. In considering whether a temporary facility or procedure change
impacts other aspects of the facility, a licensee should apply 10 CFR 50.59, paying particular
IMC0326 states, in part: Additionally, if a compensatory measure involves a temporary facility  
attention to ancillary aspects of the temporary change that result from actions taken to directly
or procedure change, 10 CFR 50.59 should be applied to the temporary change with the  
compensate for the degraded condition. Whenever degraded or nonconforming conditions
intent to determine whether the temporary change/compensatory measure itself (not the  
are discovered, 10 CFR Part 50, Appendix B, requires prompt corrective action to correct or
degraded or nonconforming condition) impacts other aspects of the facility or procedures  
resolve the condition.
described in the UFSAR. In considering whether a temporary facility or procedure change  
In summary, the discovery of an improper or inadequate TS value or required action is
impacts other aspects of the facility, a licensee should apply 10 CFR 50.59, paying particular  
considered a degraded or nonconforming condition as defined in IMC0326. Imposing
attention to ancillary aspects of the temporary change that result from actions taken to directly  
administrative controls in response to an improper or inadequate TS is considered an
compensate for the degraded condition. Whenever degraded or nonconforming conditions  
acceptable short-term corrective action. The NRC staff expects that, following the imposition
are discovered, 10 CFR Part 50, Appendix B, requires prompt corrective action to correct or  
of administrative controls, an amendment to the TS, with appropriate justification and
resolve the condition.  
schedule, will be submitted in a timely fashion. Once any amendment correcting the TS is
approved, the licensee must update the final safety analysis report, as necessary, to comply
In summary, the discovery of an improper or inadequate TS value or required action is  
with 10 CFR 50.71(e).
considered a degraded or nonconforming condition as defined in IMC0326. Imposing  
Because the licensee did not perform a 50.59 screening for the compensatory measures
administrative controls in response to an improper or inadequate TS is considered an  
associated with the restricted operating conditions, the licensee failed to recognize that the
acceptable short-term corrective action. The NRC staff expects that, following the imposition  
TSs were now non-conservative and that NRC approval was required.
of administrative controls, an amendment to the TS, with appropriate justification and  
Corrective Actions: The licensee documented the violation in the corrective action program
schedule, will be submitted in a timely fashion. Once any amendment correcting the TS is  
and created actions to review 50.59 screening requirements.
approved, the licensee must update the final safety analysis report, as necessary, to comply  
Corrective Action Reference: CR-RBS-2018-03147
with 10 CFR 50.71(e).  
Performance Assessment:
Performance Deficiency: The failure to perform a written safety evaluation for the effect of
Because the licensee did not perform a 50.59 screening for the compensatory measures  
compensatory measures implemented due to degraded feedwater sparger nozzles was a
associated with the restricted operating conditions, the licensee failed to recognize that the  
performance deficiency.
TSs were now non-conservative and that NRC approval was required.  
Screening: The performance deficiency was evaluated in accordance with the traditional
enforcement process because it impacted the ability of the NRC to perform its regulatory
Corrective Actions: The licensee documented the violation in the corrective action program  
oversight function.
and created actions to review 50.59 screening requirements.  
Significance: Using example 6.1.d.2 from the NRC Enforcement Policy, the violation was
determined to be a Severity Level IV violation.
Corrective Action Reference: CR-RBS-2018-03147  
Cross-cutting Aspect: Because the violation was dispositioned using the traditional
Performance Assessment:  
enforcement process, no cross cutting aspect was assigned.
                                                19
Performance Deficiency: The failure to perform a written safety evaluation for the effect of  
compensatory measures implemented due to degraded feedwater sparger nozzles was a  
performance deficiency.  
Screening: The performance deficiency was evaluated in accordance with the traditional  
enforcement process because it impacted the ability of the NRC to perform its regulatory  
oversight function.  
Significance: Using example 6.1.d.2 from the NRC Enforcement Policy, the violation was  
determined to be a Severity Level IV violation.  
Cross-cutting Aspect: Because the violation was dispositioned using the traditional  
enforcement process, no cross cutting aspect was assigned.  


Enforcement:
Violation: Title 10 CFR 50.59(d)(1) requires, in part, that the licensee shall maintain records
of changes in the facility, of changes in procedures, and of tests and experiments as
20
described in the updated final safety analysis report (UFSAR). These records must include a
written evaluation which provides a basis for the determination that the change, test, or
Enforcement:  
experiment does not require a license amendment.
Contrary to the above, since January 29, 2018, the licensee failed to maintain records of a
Violation: Title 10 CFR 50.59(d)(1) requires, in part, that the licensee shall maintain records  
change to the facility, as described in the UFSAR, that include a written evaluation which
of changes in the facility, of changes in procedures, and of tests and experiments as  
provides a basis for the determination that the change did not require a license amendment.
described in the updated final safety analysis report (UFSAR). These records must include a  
Specifically, the licensee made changes pursuant to 10 CFR 50.59(c) to the plant as
written evaluation which provides a basis for the determination that the change, test, or  
described in the UFSAR and did not provide a written evaluation for the determination that
experiment does not require a license amendment.  
compensatory measures prohibiting operation in single loop condition were technical
specification changes, and as such required prior NRC approval.
Contrary to the above, since January 29, 2018, the licensee failed to maintain records of a  
Disposition: This violation is being treated as an non-cited violation consistent with
change to the facility, as described in the UFSAR, that include a written evaluation which  
Section 2.3.2.a of the NRC Enforcement Policy.
provides a basis for the determination that the change did not require a license amendment.
Failure to Conduct Adequate Transient Snap Shot Assessment Following Recirculation Pump
Specifically, the licensee made changes pursuant to 10 CFR 50.59(c) to the plant as  
Trip
described in the UFSAR and did not provide a written evaluation for the determination that  
Cornerstone           Significance                               Cross-cutting     Report
compensatory measures prohibiting operation in single loop condition were technical  
                                                                  Aspect            Section
specification changes, and as such required prior NRC approval.  
Initiating Events     Green                                     None              71152 -
                      FIN 05000458/2018012-01                                     Problem
Disposition: This violation is being treated as an non-cited violation consistent with  
                      Closed                                                      Identification
Section 2.3.2.a of the NRC Enforcement Policy.  
                                                                                    and
                                                                                    Resolution
Failure to Conduct Adequate Transient Snap Shot Assessment Following Recirculation Pump  
The inspectors identified a Green finding for the licensees failure to adequately validate
Trip  
simulator response during a transient snap shot assessment following an unexpected trip of
Cornerstone  
reactor recirculation pump A on December 19, 2012.
Significance  
Description:
Cross-cutting  
On December 19, 2012, with the plant operating at 100 percent power, reactor recirculation
Aspect
pump A unexpectedly tripped off. As a result, the plant configuration consisted of one
Report  
recirculation pump running in fast speed and the other recirculation pump secured. During
Section  
this single loop configuration, station personnel identified that emergency response
Initiating Events  
information system (ERIS) point B33NA01V indicated suspect and was not available for
Green  
use. The station documented this condition in Condition Report CR-RBS-2012-07759.
FIN 05000458/2018012-01  
On February 1, 2018, with the unit in Mode 1 at approximately 27 percent power, reactor
Closed
recirculation pump B unexpectedly tripped during an upshift in the speed of the pump. As a
None
result, the reactor was in a single loop configuration with the recirculation pump A running in
71152 -
fast speed and the recirculation pump B not running. Operators entered abnormal operating
Problem  
procedure AOP-0024, Thermal Hydraulic Instability Controls, Revision 30, as a result of the
Identification  
unplanned entry into single loop operations. Step 5.8 of this procedure directed operators to
and  
determine core flow and enter general operating procedure GOP-004, Single Loop
Resolution  
Operations. Step 5.8 also instructed operators to determine core flow using process
The inspectors identified a Green finding for the licensees failure to adequately validate  
computer point B33NA01V (which can be observed in both ERIS and the plant process
simulator response during a transient snap shot assessment following an unexpected trip of  
computer) when in a configuration with one recirculation pump in fast speed and one
reactor recirculation pump A on December 19, 2012.  
                                                20
Description:  
On December 19, 2012, with the plant operating at 100 percent power, reactor recirculation  
pump A unexpectedly tripped off. As a result, the plant configuration consisted of one  
recirculation pump running in fast speed and the other recirculation pump secured. During  
this single loop configuration, station personnel identified that emergency response  
information system (ERIS) point B33NA01V indicated suspect and was not available for  
use. The station documented this condition in Condition Report CR-RBS-2012-07759.  
On February 1, 2018, with the unit in Mode 1 at approximately 27 percent power, reactor  
recirculation pump B unexpectedly tripped during an upshift in the speed of the pump. As a  
result, the reactor was in a single loop configuration with the recirculation pump A running in  
fast speed and the recirculation pump B not running. Operators entered abnormal operating  
procedure AOP-0024, Thermal Hydraulic Instability Controls, Revision 30, as a result of the  
unplanned entry into single loop operations. Step 5.8 of this procedure directed operators to  
determine core flow and enter general operating procedure GOP-004, Single Loop  
Operations. Step 5.8 also instructed operators to determine core flow using process  
computer point B33NA01V (which can be observed in both ERIS and the plant process  
computer) when in a configuration with one recirculation pump in fast speed and one  


recirculation pump off. Control room operators observed the value of this data point as
13.9 million pounds mass per hour (Mlbm/hr) of flow through the reactor core. The operators
concluded that this value was not valid since the indicated flow was much lower than
21
expected with one recirculation pump running in fast speed. The operators then observed a
value of 27.3Mlbm/hr core flow using the ERIS data point for B33NA01V. This value
recirculation pump off. Control room operators observed the value of this data point as  
appeared to be a valid number based on the single loop operation power/flow map contained
13.9 million pounds mass per hour (Mlbm/hr) of flow through the reactor core. The operators  
in AOP-0024, Attachment 2. Normal data points on ERIS are displayed with a white text, but
concluded that this value was not valid since the indicated flow was much lower than  
control room operators observed the ERIS data point displayed in a magenta color.
expected with one recirculation pump running in fast speed. The operators then observed a  
Additionally, the word suspect appeared adjacent to the data point for core flow. Control
value of 27.3Mlbm/hr core flow using the ERIS data point for B33NA01V. This value  
room operators contacted information technology personnel and attempted to understand the
appeared to be a valid number based on the single loop operation power/flow map contained  
magenta color and suspect information associated with the core flow data point.
in AOP-0024, Attachment 2. Normal data points on ERIS are displayed with a white text, but  
Concurrently, operators attempted to validate core flow using alternate means but were
control room operators observed the ERIS data point displayed in a magenta color.
unsuccessful, as the alternate indications did not provide accurate core flow readings at low
Additionally, the word suspect appeared adjacent to the data point for core flow. Control  
reactor power when in a single loop configuration. After approximately one hour spent
room operators contacted information technology personnel and attempted to understand the  
seeking to understand the unfamiliar indication associated with B33NA01V, control room
magenta color and suspect information associated with the core flow data point.
operators conducted a brief and made the decision to shut down the unit due to the
Concurrently, operators attempted to validate core flow using alternate means but were  
uncertainties associated with the core flow data point. Following plant shutdown and
unsuccessful, as the alternate indications did not provide accurate core flow readings at low  
subsequent troubleshooting and investigation, licensee personnel concluded that the
reactor power when in a single loop configuration. After approximately one hour spent  
magenta text and suspect note associated with ERIS B33NA01V was an expected system
seeking to understand the unfamiliar indication associated with B33NA01V, control room  
response. Below approximately 40 percent core flow, the plant process computer shifts the
operators conducted a brief and made the decision to shut down the unit due to the  
calculation method from the primary means of calculating core flow using the sum of jet pump
uncertainties associated with the core flow data point. Following plant shutdown and  
flows to an alternate process that uses core plate differential pressure. As a result of shifting
subsequent troubleshooting and investigation, licensee personnel concluded that the  
to the alternate calculation of core flow, data point ERIS B33NA01V was programmed to turn
magenta text and suspect note associated with ERIS B33NA01V was an expected system  
magenta in color and display suspect to alert operators that the method of calculating core
response. Below approximately 40 percent core flow, the plant process computer shifts the  
flow had changed. After this information was disseminated to licensed operators, the
calculation method from the primary means of calculating core flow using the sum of jet pump  
licensee implemented procedural changes to AOP-0024 that provided amplifying information
flows to an alternate process that uses core plate differential pressure. As a result of shifting  
regarding B33NA01V validated core flow. Specifically, the licensee revised the procedure on
to the alternate calculation of core flow, data point ERIS B33NA01V was programmed to turn  
February 7, 2018, in order to provide clear guidance regarding expected system response of
magenta in color and display suspect to alert operators that the method of calculating core  
the process computer data points during abnormal flow configurations.
flow had changed. After this information was disseminated to licensed operators, the  
The inspectors compared the actual plant response to the simulator response for the trip of a
licensee implemented procedural changes to AOP-0024 that provided amplifying information  
recirculation pump while at low power. The actual conditions in the main control room during
regarding B33NA01V validated core flow. Specifically, the licensee revised the procedure on  
the event on February 1, 2018, resulted in ERIS point B33NA01V indicating the correct flow
February 7, 2018, in order to provide clear guidance regarding expected system response of  
(27.3Mlbm/hr), but the data point turned magenta in color and displayed the warning label
the process computer data points during abnormal flow configurations.  
suspect. This was later determined by information technology personnel to be the correct
response and data display, and was the result of the core flow calculation methodology
The inspectors compared the actual plant response to the simulator response for the trip of a  
swapping from the primary method (jet pump flow) to the alternate method (core plate
recirculation pump while at low power. The actual conditions in the main control room during  
differential pressure).
the event on February 1, 2018, resulted in ERIS point B33NA01V indicating the correct flow  
In the simulator, the inspectors determined that ERIS point B33NA01V provided erratic
(27.3Mlbm/hr), but the data point turned magenta in color and displayed the warning label  
indications of core flow following a simulated trip of the recirculation pump B from an initial
suspect. This was later determined by information technology personnel to be the correct  
condition of approximately 25 percent. The indicated flow varied, and ultimately stabilized at
response and data display, and was the result of the core flow calculation methodology  
approximately 10Mlbm/hr, which is less than half of the expected indication. Additionally,
swapping from the primary method (jet pump flow) to the alternate method (core plate  
B33NA01V did not change to a magenta color, and it did not display the word suspect. The
differential pressure).  
inspectors determined that ERIS B33NA01V was programmed to calculate core flow using
the sum of jet pump flows at all power levels. As a result, the displayed value was inaccurate
In the simulator, the inspectors determined that ERIS point B33NA01V provided erratic  
below 40 percent core flow, and the data point was not programmed to turn magenta or
indications of core flow following a simulated trip of the recirculation pump B from an initial  
indicate suspect since no swap to a backup means of calculation below 40 percent core
condition of approximately 25 percent. The indicated flow varied, and ultimately stabilized at  
flow was modelled.
approximately 10Mlbm/hr, which is less than half of the expected indication. Additionally,  
                                                21
B33NA01V did not change to a magenta color, and it did not display the word suspect. The  
inspectors determined that ERIS B33NA01V was programmed to calculate core flow using  
the sum of jet pump flows at all power levels. As a result, the displayed value was inaccurate  
below 40 percent core flow, and the data point was not programmed to turn magenta or  
indicate suspect since no swap to a backup means of calculation below 40 percent core  
flow was modelled.  


The inspectors reviewed procedure EN-OP-117, Operations Assessments, Version 4,
Section 5.4, which states that transient snap-shot assessments are performed whenever a
plant transient occurs. A plant transient is defined in section 5.4[2] as including any turbine
22
generator power change in excess of 10 percent of rated power in less than one minute other
than a momentary spike due to a grid disturbance or a manually initiated runback. The
The inspectors reviewed procedure EN-OP-117, Operations Assessments, Version 4,  
inspectors concluded that the recirculation pump A trip on December 19, 2012, met the
Section 5.4, which states that transient snap-shot assessments are performed whenever a  
definition of a transient. EN-OP-117, Attachment 9.2, Transient Snap Shot Assessment
plant transient occurs. A plant transient is defined in section 5.4[2] as including any turbine  
Documentation Form, Objective 7, discusses the training preparation aspect of the
generator power change in excess of 10 percent of rated power in less than one minute other  
assessment. Specifically, the transient snap-shot assessment is performed in order to
than a momentary spike due to a grid disturbance or a manually initiated runback. The  
validate that the simulator accurately represented the plant characteristics of the transient.
inspectors concluded that the recirculation pump A trip on December 19, 2012, met the  
The licensee provided a Post-Event Simulator Test report that was run on February 14, 2013.
definition of a transient. EN-OP-117, Attachment 9.2, Transient Snap Shot Assessment  
The report concluded that the simulator response matched the parameters observed in the
Documentation Form, Objective 7, discusses the training preparation aspect of the  
plant. The inspectors determined that although the snap-shot assessment was performed,
assessment. Specifically, the transient snap-shot assessment is performed in order to  
station personnel did not validate that ERIS B33NA01V (validated core flow) provided
validate that the simulator accurately represented the plant characteristics of the transient.
operators with the same indications seen by operators in the plant during a recirculation
The licensee provided a Post-Event Simulator Test report that was run on February 14, 2013.
pump trip.
The report concluded that the simulator response matched the parameters observed in the  
The inspectors determined that no condition report or simulator deficiency report was
plant. The inspectors determined that although the snap-shot assessment was performed,  
generated to document the discrepancy between the plant and the simulator for displaying
station personnel did not validate that ERIS B33NA01V (validated core flow) provided  
ERIS B33NA01V. The simulator ERIS B33NA01V core flow indication did not display the
operators with the same indications seen by operators in the plant during a recirculation  
correct value for core flow and also did not indicate suspect or turn magenta. The
pump trip.  
inspectors reviewed training documentation to determine why this discrepancy was not
observed during continuing simulator training scenarios. The inspectors concluded that this
The inspectors determined that no condition report or simulator deficiency report was  
discrepancy was not documented because the station did not conduct training on abnormal
generated to document the discrepancy between the plant and the simulator for displaying  
single loop operations during low power operations. The inspectors reviewed industry
ERIS B33NA01V. The simulator ERIS B33NA01V core flow indication did not display the  
standards and guidelines for simulator training and determined that the station is required to
correct value for core flow and also did not indicate suspect or turn magenta. The  
periodically conduct training on abnormal events that occur during low power operations.
inspectors reviewed training documentation to determine why this discrepancy was not  
Corrective Actions: The station documented the core flow indication simulator deficiency in a
observed during continuing simulator training scenarios. The inspectors concluded that this  
deficiency report and generated actions to incorporate the discrepancy into future licensed
discrepancy was not documented because the station did not conduct training on abnormal  
operator training sessions.
single loop operations during low power operations. The inspectors reviewed industry  
Corrective Action Reference: CR-RBS-2018-03145
standards and guidelines for simulator training and determined that the station is required to  
Performance Assessment:
periodically conduct training on abnormal events that occur during low power operations.  
Performance Deficiency: The licensees failure to validate core flow in the simulator during a
transient snap shot assessment following the trip of the reactor recirculation pump A on
Corrective Actions: The station documented the core flow indication simulator deficiency in a  
December 19, 2012, was a performance deficiency.
deficiency report and generated actions to incorporate the discrepancy into future licensed  
Screening: The performance deficiency was more than minor, and therefore a finding,
operator training sessions.  
because it was associated with the human performance attribute of the Initiating Events
Cornerstone and adversely affected the cornerstone objective to limit the likelihood of events
Corrective Action Reference: CR-RBS-2018-03145  
that upset plant stability and challenge critical safety functions during shutdown as well as
Performance Assessment:  
power operations. Specifically, the failure to validate simulator fidelity following a plant
transient prevented the licensee from identifying simulator model discrepancies when
Performance Deficiency: The licensees failure to validate core flow in the simulator during a  
determining core flow during low power, single loop operations.
transient snap shot assessment following the trip of the reactor recirculation pump A on  
                                                22
December 19, 2012, was a performance deficiency.  
Screening: The performance deficiency was more than minor, and therefore a finding,  
because it was associated with the human performance attribute of the Initiating Events  
Cornerstone and adversely affected the cornerstone objective to limit the likelihood of events  
that upset plant stability and challenge critical safety functions during shutdown as well as  
power operations. Specifically, the failure to validate simulator fidelity following a plant  
transient prevented the licensee from identifying simulator model discrepancies when  
determining core flow during low power, single loop operations.  


Significance: The inspectors screened the finding in accordance with Inspection Manual
Chapter 0609, Appendix A, The Significance Determination Process for Findings At-Power.
The finding was determined to be of very low safety significance (Green) because the finding
23
did not contribute to both the likelihood of a reactor trip and the likelihood that mitigating
equipment would not be available.
Significance: The inspectors screened the finding in accordance with Inspection Manual  
Cross-cutting Aspect: No cross cutting aspect was assigned because the performance
Chapter 0609, Appendix A, The Significance Determination Process for Findings At-Power.
deficiency is not indicative of current licensee performance.
The finding was determined to be of very low safety significance (Green) because the finding  
Enforcement: Inspectors did not identify a violation of regulatory requirements associated
did not contribute to both the likelihood of a reactor trip and the likelihood that mitigating  
with this finding.
equipment would not be available.  
Failure to Submit a Licensee Event Report for a Manual Scram
Cornerstone         Significance                                     Cross-cutting   Report
Cross-cutting Aspect: No cross cutting aspect was assigned because the performance  
                                                                    Aspect          Section
deficiency is not indicative of current licensee performance.  
None               SLIV                                             None            71153 -
Enforcement: Inspectors did not identify a violation of regulatory requirements associated  
                    NCV 05000458/2018012-04                                           Follow-up of
with this finding.  
                    Closed                                                            Events and
                                                                                      Notices of
Failure to Submit a Licensee Event Report for a Manual Scram  
                                                                                      Enforcement
Cornerstone  
                                                                                      Discretion
Significance  
The inspectors identified a Severity Level IV non-cited violation of 10 CFR 50.73, Licensee
Cross-cutting  
Event Report System, for the licensees failure to submit a required licensee event report
Aspect
(LER). Specifically, on February 1, 2018, after an unexpected trip of the recirculation pump
Report  
B, the licensee initiated a manual scram of the reactor that was not part of a preplanned
Section  
sequence and failed to submit an LER within 60 days.
None  
Description: At approximately 9:46 a.m. on February 1, 2018, with the unit operating at
SLIV  
approximately 27 percent power, the recirculation pump B unexpectedly tripped during an
NCV 05000458/2018012-04  
attempted transfer from slow to fast speed. The licensee promptly entered AOP-0024,
Closed
Thermal Hydraulic Instability, and GOP-0004, Single Loop Operation. Note 5.8 of AOP-
None
0024 and Precaution 3.6 of GOP-0004 instruct the licensee to use process computer point
71153 -
B33NA01V to determine core flow while in single loop operation. The plant process computer
Follow-up of  
(PPC) and emergency response information system (ERIS) readouts showed conflicting
Events and  
indications for this computer point, with the PPC showing approximately 13,900 Mlbm/hr of
Notices of  
flow and ERIS showing approximately 26,000 Mlbm/hr of flow.
Enforcement  
Step 5.1 of AOP-0024 instructs the licensee to determine where on the power-to-flow map the
Discretion  
plant is operating. If the plant is operating in the restricted region, the procedure states to exit
The inspectors identified a Severity Level IV non-cited violation of 10 CFR 50.73, Licensee  
that region by lowering power or raising flow. If the plant is operating in the exclusion region,
Event Report System, for the licensees failure to submit a required licensee event report  
the procedure states to verify that a scram has occurred. The indicated PPC value for core
(LER). Specifically, on February 1, 2018, after an unexpected trip of the recirculation pump  
flow put the plant in an unanalyzed region of the power-to-flow map, with less flow than the
B, the licensee initiated a manual scram of the reactor that was not part of a preplanned  
minimum amount of flow that defines any region, including the exclusion region. The
sequence and failed to submit an LER within 60 days.  
indicated ERIS value put the plant in the restricted region, just above the boundary that
Description: At approximately 9:46 a.m. on February 1, 2018, with the unit operating at  
delineates the restricted region from the monitoring region.
approximately 27 percent power, the recirculation pump B unexpectedly tripped during an  
The licensee initially believed the ERIS value to be the correct value; however, this value was
attempted transfer from slow to fast speed. The licensee promptly entered AOP-0024,  
accompanied by a magenta suspect note on the ERIS screen, which caused the licensee to
Thermal Hydraulic Instability, and GOP-0004, Single Loop Operation. Note 5.8 of AOP-
question its validity. In an effort to determine the true value of core flow, the licensee
0024 and Precaution 3.6 of GOP-0004 instruct the licensee to use process computer point  
performed a manual calculation using other known inputs. The licensee performed this
B33NA01V to determine core flow while in single loop operation. The plant process computer  
calculation incorrectly and wrongly corroborated the PPC value as the correct value. Given
(PPC) and emergency response information system (ERIS) readouts showed conflicting  
indications for this computer point, with the PPC showing approximately 13,900 Mlbm/hr of  
flow and ERIS showing approximately 26,000 Mlbm/hr of flow.  
Step 5.1 of AOP-0024 instructs the licensee to determine where on the power-to-flow map the  
plant is operating. If the plant is operating in the restricted region, the procedure states to exit  
that region by lowering power or raising flow. If the plant is operating in the exclusion region,  
the procedure states to verify that a scram has occurred. The indicated PPC value for core  
flow put the plant in an unanalyzed region of the power-to-flow map, with less flow than the  
minimum amount of flow that defines any region, including the exclusion region. The  
indicated ERIS value put the plant in the restricted region, just above the boundary that  
delineates the restricted region from the monitoring region.  
The licensee initially believed the ERIS value to be the correct value; however, this value was  
accompanied by a magenta suspect note on the ERIS screen, which caused the licensee to  
question its validity. In an effort to determine the true value of core flow, the licensee  
performed a manual calculation using other known inputs. The licensee performed this  
calculation incorrectly and wrongly corroborated the PPC value as the correct value. Given  
the inability to establish that the plant was operating in any allowed region of the power-to-
the inability to establish that the plant was operating in any allowed region of the power-to-
                                                  23


flow map, the licensee made the decision to manually actuate the reactor protection system
(RPS) by taking the reactor mode switch to shutdown.
During the investigation after the scram, the licensee determined that the ERIS value was, in
24
fact, a valid indication of core flow at the time of the event. Operators had not been
adequately trained on the meaning of the magenta suspect indication, and were therefore
flow map, the licensee made the decision to manually actuate the reactor protection system  
unable to determine the implications of the indications on the validity of the data point.
(RPS) by taking the reactor mode switch to shutdown.  
Pursuant to the requirements of 10 CFR 50.72(b)(3)(iv), the licensee reported the scram
event to the NRC at 1:23 p.m. as an event that resulted in an actuation of the RPS. On
During the investigation after the scram, the licensee determined that the ERIS value was, in  
March 23, 2018, the licensee retracted the report on the grounds that the actuation was part
fact, a valid indication of core flow at the time of the event. Operators had not been  
of a pre-planned sequence during testing or reactor operation. The inspectors concluded that
adequately trained on the meaning of the magenta suspect indication, and were therefore  
this retraction was inappropriate and that the event was reportable for the reasons provided
unable to determine the implications of the indications on the validity of the data point.  
below.
The inspectors reviewed NUREG-1022, Event Report Guidelines 10 CFR 50.72 and 50.73,
Pursuant to the requirements of 10 CFR 50.72(b)(3)(iv), the licensee reported the scram  
revision 3, which provides the following guidance: Actuations that need not be reported are
event to the NRC at 1:23 p.m. as an event that resulted in an actuation of the RPS. On  
those initiated for reasons other than to mitigate the consequences of an event (e.g., at the
March 23, 2018, the licensee retracted the report on the grounds that the actuation was part  
discretion of the licensee as part of a preplanned procedure). In the case of the February 1,
of a pre-planned sequence during testing or reactor operation. The inspectors concluded that  
2018, River Bend scram event, the inspectors determined that the manual RPS actuation was
this retraction was inappropriate and that the event was reportable for the reasons provided  
initiated in order to mitigate the consequences (i.e., uncertainty as to the condition of the plant
below.  
with respect to core flow and power-to-flow considerations) of an event (i.e., the unexpected
The inspectors reviewed NUREG-1022, Event Report Guidelines 10 CFR 50.72 and 50.73,  
loss of a reactor recirculation pump).
revision 3, which provides the following guidance: Actuations that need not be reported are  
NUREG-1022 also provides an example of a reportable manual scram that was event driven
those initiated for reasons other than to mitigate the consequences of an event (e.g., at the  
and not part of a preplanned sequence during testing or reactor operation:
discretion of the licensee as part of a preplanned procedure). In the case of the February 1,  
        At a BWR, both recirculation pumps tripped as a result of a breaker problem. This
2018, River Bend scram event, the inspectors determined that the manual RPS actuation was  
        placed the plant in a condition in which BWRs are typically scrammed to avoid
initiated in order to mitigate the consequences (i.e., uncertainty as to the condition of the plant  
        potential power/flow oscillations. At this plant, for this condition, a written off-normal
with respect to core flow and power-to-flow considerations) of an event (i.e., the unexpected  
        procedure required the plant operations staff to scram the reactor. The plant staff
loss of a reactor recirculation pump).    
        performed a reactor scram, which was uncomplicated. This event is reportable as a
        manual RPS actuation. Even though the reactor scram was in response to an existing
NUREG-1022 also provides an example of a reportable manual scram that was event driven  
        written procedure, this event does not involve a preplanned sequence because the
and not part of a preplanned sequence during testing or reactor operation:
        loss of recirculation pumps and the resultant off-normal procedure entry were event
        driven, not preplanned. Both an ENS notification and an LER are required. In this
At a BWR, both recirculation pumps tripped as a result of a breaker problem. This  
        case, the licensee initially retracted the ENS notification, believing that the event was
placed the plant in a condition in which BWRs are typically scrammed to avoid  
        not reportable. After staff review and further discussion, it was agreed that the event
potential power/flow oscillations. At this plant, for this condition, a written off-normal  
        is reportable for the reasons discussed above.
procedure required the plant operations staff to scram the reactor. The plant staff  
As with the scram in the above example, the scram that occurred at River Bend Station was
performed a reactor scram, which was uncomplicated. This event is reportable as a  
not part of a preplanned sequence during testing or reactor operation, but was instead an
manual RPS actuation. Even though the reactor scram was in response to an existing  
event driven response to a series of unplanned and unexpected adverse occurrences in the
written procedure, this event does not involve a preplanned sequence because the  
plant. These occurrences included: a trip of the recirculation pump B, entry into an abnormal
loss of recirculation pumps and the resultant off-normal procedure entry were event  
operating procedure for thermal hydraulic instability, an inability to determine core flow and
driven, not preplanned. Both an ENS notification and an LER are required. In this  
location on the power-to-flow map in accordance with that procedure, a realization that the
case, the licensee initially retracted the ENS notification, believing that the event was  
PPC indication of core flow put the plant outside of any allowed operating region of the
not reportable. After staff review and further discussion, it was agreed that the event  
power-to-flow map, an incorrect manual calculation that wrongly corroborated the accuracy of
is reportable for the reasons discussed above.  
the PPC indication, and the presence of a poorly understood suspect indication that
appeared to undermine the validity of the ERIS flow indication. These adverse occurrences
As with the scram in the above example, the scram that occurred at River Bend Station was  
generated uncertainty as to the status of reactor safety. The subsequent decision to perform
not part of a preplanned sequence during testing or reactor operation, but was instead an  
                                                  24
event driven response to a series of unplanned and unexpected adverse occurrences in the  
plant. These occurrences included: a trip of the recirculation pump B, entry into an abnormal  
operating procedure for thermal hydraulic instability, an inability to determine core flow and  
location on the power-to-flow map in accordance with that procedure, a realization that the  
PPC indication of core flow put the plant outside of any allowed operating region of the  
power-to-flow map, an incorrect manual calculation that wrongly corroborated the accuracy of  
the PPC indication, and the presence of a poorly understood suspect indication that  
appeared to undermine the validity of the ERIS flow indication. These adverse occurrences  
generated uncertainty as to the status of reactor safety. The subsequent decision to perform  


a manual reactor scram was consistent with general instruction provided in EN-OP-115,
Conduct of Operations, which states: do not hesitate to reduce power or perform an
immediate reactor shutdown when reactor safety is uncertain. As with the scram in the
25
a manual reactor scram was consistent with general instruction provided in EN-OP-115,  
Conduct of Operations, which states: do not hesitate to reduce power or perform an  
immediate reactor shutdown when reactor safety is uncertain. As with the scram in the  
above example, the February 1, 2018, River Bend scram also involved entry into an off-
above example, the February 1, 2018, River Bend scram also involved entry into an off-
normal procedure due to an unexpected plant equipment malfunction that resulted in the
normal procedure due to an unexpected plant equipment malfunction that resulted in the  
potential for the plant to be in an undesired condition with respect to power-to-flow
potential for the plant to be in an undesired condition with respect to power-to-flow  
considerations.
considerations.
The senior resident inspector was present in the control room during the events and was able
to confirm that the shutdown was event driven rather than preplanned. At 10:55 a.m., the
The senior resident inspector was present in the control room during the events and was able  
control room briefed that because PPC and ERIS showed conflicting indications of core flow
to confirm that the shutdown was event driven rather than preplanned. At 10:55 a.m., the  
with ERIS indicating suspect, the mode switch was going to be placed in shutdown. At
control room briefed that because PPC and ERIS showed conflicting indications of core flow  
10:57 a.m., roughly two minutes after the brief was completed, the reactor operator
with ERIS indicating suspect, the mode switch was going to be placed in shutdown. At  
scrammed the reactor, and the following station log entry was made: MCR [main control
10:57 a.m., roughly two minutes after the brief was completed, the reactor operator  
room] announces placing plant in shut down due to inability to regulate recirculation flow. If
scrammed the reactor, and the following station log entry was made: MCR [main control  
the reactor shutdown had been preplanned, it would not have proceeded at this accelerated
room] announces placing plant in shut down due to inability to regulate recirculation flow. If  
pace. Rather, the licensee would have worked through the relevant steps of the applicable
the reactor shutdown had been preplanned, it would not have proceeded at this accelerated  
shutdown procedure, GOP-0004, Single Loop Operation, scramming the reactor only after
pace. Rather, the licensee would have worked through the relevant steps of the applicable  
those steps had been completed and signed for. Upon review of the copy of GOP-0004 that
shutdown procedure, GOP-0004, Single Loop Operation, scramming the reactor only after  
was in use by the operators on February 1, 2018, the inspectors noted that no steps of
those steps had been completed and signed for. Upon review of the copy of GOP-0004 that  
Attachment 3, Shutdown from Single Loop Operation, were marked as completed, and the
was in use by the operators on February 1, 2018, the inspectors noted that no steps of  
attachment was not signed off as being initiated or completed. The deviation from normal
Attachment 3, Shutdown from Single Loop Operation, were marked as completed, and the  
practice was appropriate because the scram was not being initiated as part of a preplanned
attachment was not signed off as being initiated or completed. The deviation from normal  
sequence. It was instead being initiated in response to the unanticipated emergence of a
practice was appropriate because the scram was not being initiated as part of a preplanned  
safety concern.
sequence. It was instead being initiated in response to the unanticipated emergence of a  
Corrective Actions: The licensee documented the violation in the corrective action program
safety concern.  
and generated corrective actions to review reportability requirements.
Corrective Action Reference(s): CR-RBS-2018-03953
Corrective Actions: The licensee documented the violation in the corrective action program  
Performance Assessment:
and generated corrective actions to review reportability requirements.  
Performance Deficiency: The failure to submit a required licensee event report was a
performance deficiency.
Corrective Action Reference(s): CR-RBS-2018-03953  
Screening: The performance deficiency was evaluated in accordance with the reactor
Performance Assessment:  
oversight process and was determined to be minor because it could not be reasonably
viewed as a precursor to a significant event, would not have the potential to lead to a more
Performance Deficiency: The failure to submit a required licensee event report was a  
significant safety concern, does not relate to a performance indicator that would have caused
performance deficiency.  
the performance indicator to exceed a threshold, and did not adversely affect a cornerstone
objective. The performance deficiency was evaluated in accordance with the traditional
Screening: The performance deficiency was evaluated in accordance with the reactor  
enforcement process because it impacted the ability of the NRC to perform its regulatory
oversight process and was determined to be minor because it could not be reasonably  
oversight function.
viewed as a precursor to a significant event, would not have the potential to lead to a more  
Significance: Using example 6.9.d.9 from the NRC Enforcement Policy, the violation was
significant safety concern, does not relate to a performance indicator that would have caused  
determined to be a Severity Level IV violation.
the performance indicator to exceed a threshold, and did not adversely affect a cornerstone  
Cross-cutting Aspect: Because the violation was dispositioned using the traditional
objective. The performance deficiency was evaluated in accordance with the traditional  
enforcement process, no cross-cutting aspect was assigned.
enforcement process because it impacted the ability of the NRC to perform its regulatory  
                                                25
oversight function.  
Significance: Using example 6.9.d.9 from the NRC Enforcement Policy, the violation was  
determined to be a Severity Level IV violation.  
Cross-cutting Aspect: Because the violation was dispositioned using the traditional  
enforcement process, no cross-cutting aspect was assigned.  


  Enforcement:
   
  Violation: 10 CFR 50.73(a)(1) requires, in part, that the licensee shall submit a Licensee
Event Report (LER) for any event of the type described in this paragraph within 60 days after
26
the discovery of the event. 10 CFR 50.73(a)(2)(iv)(A) requires, in part, that the licensee shall
report any event or condition that resulted in manual actuation of the reactor protection
Enforcement:  
system (RPS) except when the actuation resulted from and was part of a pre-planned
   
sequence during testing or reactor operation. Contrary to the above, on April 2, 2018, the
Violation: 10 CFR 50.73(a)(1) requires, in part, that the licensee shall submit a Licensee  
licensee failed to submit an LER within 60 days after the discovery of an event or condition
Event Report (LER) for any event of the type described in this paragraph within 60 days after  
that resulted in manual actuation of the RPS that did not result from and that was not a part of
the discovery of the event. 10 CFR 50.73(a)(2)(iv)(A) requires, in part, that the licensee shall  
a pre-planned sequence during testing or reactor operation. Specifically, the licensee failed
report any event or condition that resulted in manual actuation of the reactor protection  
to submit an LER within 60 days of a manual reactor scram that occurred on February 1,
system (RPS) except when the actuation resulted from and was part of a pre-planned  
2018.
sequence during testing or reactor operation. Contrary to the above, on April 2, 2018, the  
Disposition: Because this SLIV violation was neither repetitive nor willful, and because it was
licensee failed to submit an LER within 60 days after the discovery of an event or condition  
entered into the licensees corrective action program as Condition Report
that resulted in manual actuation of the RPS that did not result from and that was not a part of  
CR-RBS-2018-03953, it is being treated as a non-cited violation consistent with
a pre-planned sequence during testing or reactor operation. Specifically, the licensee failed  
Section 2.3.2.a of the NRC Enforcement Policy.
to submit an LER within 60 days of a manual reactor scram that occurred on February 1,  
EXIT MEETINGS AND DEBRIEFS
2018.  
The inspectors verified no proprietary information was retained or documented in this report.
Disposition: Because this SLIV violation was neither repetitive nor willful, and because it was  
On May 31, 2018, and on July 16, 2018, the inspectors presented the inspection results to
entered into the licensees corrective action program as Condition Report  
Mr. W. Maguire, Site Vice President, and other members of the licensee staff.
CR-RBS-2018-03953, it is being treated as a non-cited violation consistent with  
                                                26
Section 2.3.2.a of the NRC Enforcement Policy.  
EXIT MEETINGS AND DEBRIEFS  
The inspectors verified no proprietary information was retained or documented in this report.  
On May 31, 2018, and on July 16, 2018, the inspectors presented the inspection results to  
Mr. W. Maguire, Site Vice President, and other members of the licensee staff.  


DOCUMENTS REVIEWED
71111.15Operability Determinations and Functionality Assessments
Procedures
Number                 Title                                                   Revision
Attachment
EN-OE-100             Operating Experience Program                           12 & 13
DOCUMENTS REVIEWED  
STP-051-4206           (RPS Bypassed) RPS/RHR Reactor Vessel Level-Low,       305
71111.15Operability Determinations and Functionality Assessments  
                        Level 3, High, Level 8, Channel Calibration and Logic
Procedures  
                        System Functional Test (B21-N680B, B21-N683B, B21-
Number  
                        N080B)
Title  
STP-051-4227           ECCS/RCIC Actuation Ads Trip System B Reactor         20
Revision  
                        Vessel Water Level Low, Level 3/High, Level 8 Channel
EN-OE-100  
                        Calibration, and Logic System Functional Test (B21-
Operating Experience Program  
                        N095B, B21-N695B, B21-N693B)
12 & 13  
STP-501-4202           FWS/MAIN Turbine Trip System - Reactor Vessel Water     15
STP-051-4206  
                        Level - High Level 8, Channel Calibration and LSFT
(RPS Bypassed) RPS/RHR Reactor Vessel Level-Low,  
                        (C33-N004B, C33-K624B, C33-R606B, C33-K650-3)
Level 3, High, Level 8, Channel Calibration and Logic  
  G13.18.6.1.B21         Reactor Vessel Water Level - Low, Level 3 Trip Function 3
System Functional Test (B21-N680B, B21-N683B, B21-
G13.18.6.1.B21*003 Reactor Vessel Water Level - Low, Level 3 Trip Function     3
N080B)  
G13.18.6.1.B21*010 Reactor Vessel Water Level - Low, Level 8 Narrow           0, 1, 2, & 3
305
                        Range
STP-051-4227  
MCP-IC-501-4202       FWS/FEED Pump Trip System (MSO) - Reactor Vessel       0
ECCS/RCIC Actuation Ads Trip System B Reactor  
                        Water Level - High Level 8, Loop Calibration (C33-
Vessel Water Level Low, Level 3/High, Level 8 Channel  
                        LTN006B, C33-ESN606B)
Calibration, and Logic System Functional Test (B21-
71111.18Plant Modifications
N095B, B21-N695B, B21-N693B)  
Condition Reports (CR-RBS-)
20
CR-RBS-2014-05194         CR-RBS-2014-06685       CR-RBS-2014-06691     CR-RBS-2015-03253
STP-501-4202  
CR-RBS-2015-03983         CR-RBS-2015-04065       CR-RBS-2015-04117     CR-RBS-2015-08476
FWS/MAIN Turbine Trip System - Reactor Vessel Water  
CR-RBS-2015-08515         CR-RBS-2016-00791       CR-RBS-2016-00893     CR-RBS-2016-00893
Level - High Level 8, Channel Calibration and LSFT  
CR-RBS-2016-04351         CR-RBS-2016-04353       CR-RBS-2017-02828     OE-NOE-2004-00008
(C33-N004B, C33-K624B, C33-R606B, C33-K650-3)  
OE-NOE-2004-00084
15
  Engineering Changes
Number             Title                                                       Revision
EC-75588           Accept As-Is Evaluation for Remainder of Cycle 20: Sparger 0 & 1
   
                    N4C Nozzles 7 and 8 Damaged
G13.18.6.1.B21  
                                                                                  Attachment
Reactor Vessel Water Level - Low, Level 3 Trip Function  
3  
G13.18.6.1.B21*003 Reactor Vessel Water Level - Low, Level 3 Trip Function  
3  
G13.18.6.1.B21*010 Reactor Vessel Water Level - Low, Level 8 Narrow  
Range
0, 1, 2, & 3  
MCP-IC-501-4202  
FWS/FEED Pump Trip System (MSO) - Reactor Vessel  
Water Level - High Level 8, Loop Calibration (C33-
LTN006B, C33-ESN606B)  
0
71111.18Plant Modifications  
Condition Reports (CR-RBS-)  
CR-RBS-2014-05194  
CR-RBS-2014-06685  
CR-RBS-2014-06691  
CR-RBS-2015-03253  
CR-RBS-2015-03983  
CR-RBS-2015-04065  
CR-RBS-2015-04117  
CR-RBS-2015-08476  
CR-RBS-2015-08515  
CR-RBS-2016-00791  
CR-RBS-2016-00893  
CR-RBS-2016-00893  
CR-RBS-2016-04351  
CR-RBS-2016-04353  
CR-RBS-2017-02828  
OE-NOE-2004-00008  
OE-NOE-2004-00084  
   
Engineering Changes  
Number  
Title  
Revision  
EC-75588  
Accept As-Is Evaluation for Remainder of Cycle 20: Sparger  
N4C Nozzles 7 and 8 Damaged  
0 & 1


  Procedures
   
Number           Title                                                     Revision
OSP-0053         Emergency and Transient Response Support Procedure       20-25
A-2
STP-000-0001     Daily Operating Logs                                     082
DBR-0035279       GEH Comment Resolution Form                               0
4221.110-000-     Operability Assessment of the River Bend Station         0
Procedures  
043              Feedwater Sparger Assembly in the January 2018 As-
Number  
                  Found Condition
Title  
71152 - Problem Identification and Resolution
Revision  
Condition Reports (CR-RBS-)
OSP-0053  
CR-RBS-2018-00358       CR-RBS-2018-00613         CR-RBS-2018-00633   CR-RBS-2018-00733
Emergency and Transient Response Support Procedure  
CR-RBS-2018-00895       CR-RBS-2018-00294         OE-NOE-2004-00008   OE-NOE-2004-00084
20-25  
  Engineering Changes
STP-000-0001  
Number                 Title                                             Revision
Daily Operating Logs  
  EC-75663               Loose Parts Evaluation for Material Lost From     0
082  
                        Feedwater Spargers Identified During PO-18-01
DBR-0035279  
                        Foreign Material FME LPA-000
GEH Comment Resolution Form  
  Miscellaneous Documents
0  
Number                     Title                                         Revision/Date
4221.110-000-
                            OSRC Meeting 2018-0001 Minutes
043
                            OSRC Meeting 2018-0002 Minutes
Operability Assessment of the River Bend Station  
                            Action Item OE33308-20110507-A2-RBS-001
Feedwater Sparger Assembly in the January 2018 As-
  CNR RBS PO-18-01-01 Foreign Material Customer Notification Report       0
Found Condition  
ECH-NE-17-00039           River Bend MOC-20a Fuel Inspection Plan       0
0
NEDC-31336P-A             General Electric Instrument Setpoint         0
                            Methodology
NEDE-21821-A               Boiling Water Reactor Feedwater               0
                            Nozzle/Sparger Final Report
NEI 96-07                 Guidelines for 10 CFR 50.59 Implementation   1
71152 - Problem Identification and Resolution  
OE33308-20110507           Sampling Probe Found in Feedwater Sparger     August 17, 2011
Condition Reports (CR-RBS-)  
                                                A-2
CR-RBS-2018-00358  
CR-RBS-2018-00613  
CR-RBS-2018-00633  
CR-RBS-2018-00733  
CR-RBS-2018-00895  
CR-RBS-2018-00294  
OE-NOE-2004-00008  
OE-NOE-2004-00084  
   
Engineering Changes  
Number  
Title  
Revision  
   
EC-75663  
Loose Parts Evaluation for Material Lost From  
Feedwater Spargers Identified During PO-18-01  
Foreign Material FME LPA-000
0  
   
Miscellaneous Documents  
Number  
Title  
Revision/Date  
OSRC Meeting 2018-0001 Minutes  
OSRC Meeting 2018-0002 Minutes  
Action Item OE33308-20110507-A2-RBS-001  
   
CNR RBS PO-18-01-01 Foreign Material Customer Notification Report  
0  
ECH-NE-17-00039  
River Bend MOC-20a Fuel Inspection Plan  
0  
NEDC-31336P-A  
General Electric Instrument Setpoint  
Methodology  
0
NEDE-21821-A  
Boiling Water Reactor Feedwater  
Nozzle/Sparger Final Report  
0
NEI 96-07  
Guidelines for 10 CFR 50.59 Implementation  
1  
OE33308-20110507  
Sampling Probe Found in Feedwater Sparger  
August 17, 2011  


  Miscellaneous Documents
   
Number                     Title                                     Revision/Date
PO 18-01                   BOP Foreign Material Inspection Report
A-3
  RBS-ER-99-0539             Engineering Response Associated with Loose 0
                            Part in the Feedwater System
Miscellaneous Documents  
  Procedures
Number  
Number                 Title                                         Revision
Title  
AOP-0001               Reactor Scram                                 37
Revision/Date  
AOP-0024               Thermal Hydraulic Stability Controls           30, 31, & 32
PO 18-01  
EN-NF-102             Corporate Fuel Reliability                     6
BOP Foreign Material Inspection Report  
EN-OP-104             Operability Determination Process             14
   
EN-OP-111             Operational Decision Making Issue Process     15
RBS-ER-99-0539  
EN-OP-117             Operations Assessments                         4
Engineering Response Associated with Loose  
EOP-0001               Emergency Operating Procedure - RPV Control   28
Part in the Feedwater System  
GOP-0001               Plant Startup                                 99
0
GOP-0002               Power Decrease/Plant Shutdown                 78
   
GOP-0003               Scram Recovery                                 31
Procedures  
GOP-0004               Single Loop Operation                         25
Number  
OE-100                 Operating Experience Program                   1
Title  
R-PL-012               Corrective Action Program                     1
Revision  
STP-000-0001           Daily Operating Logs                           082
AOP-0001  
  Work Order
Reactor Scram  
  52599498
37  
71153Follow-up of Events and Notices of Enforcement Discretion
AOP-0024  
Procedures
Thermal Hydraulic Stability Controls  
Number           Title                                                   Revision
30, 31, & 32  
EN-OP-115         Conduct of Operations                                   23
EN-NF-102  
GOP-0004         Single Loop Operation                                   23
Corporate Fuel Reliability  
  Condition Reports (CR-RBS-)
6  
2018-03149             2018-03953
EN-OP-104  
                                              A-3
Operability Determination Process  
14  
EN-OP-111  
Operational Decision Making Issue Process  
15  
EN-OP-117  
Operations Assessments  
4  
EOP-0001  
Emergency Operating Procedure - RPV Control  
28  
GOP-0001  
Plant Startup  
99  
GOP-0002  
Power Decrease/Plant Shutdown  
78  
GOP-0003  
Scram Recovery  
31  
GOP-0004  
Single Loop Operation  
25  
OE-100  
Operating Experience Program  
1  
R-PL-012  
Corrective Action Program  
1  
STP-000-0001  
Daily Operating Logs  
082  
   
Work Order  
52599498
   
71153Follow-up of Events and Notices of Enforcement Discretion  
Procedures  
Number  
Title  
Revision  
EN-OP-115  
Conduct of Operations  
23  
GOP-0004  
Single Loop Operation  
23  
   
Condition Reports (CR-RBS-)  
2018-03149  
2018-03953  




  ML18194A413
  ML18194A413  
  SUNSI Review:       ADAMS:           Non-Publicly Available     Non-Sensitive   Keyword:
  SUNSI Review:  
  By: CHY/RDR         Yes No       Publicly Available           Sensitive     NRC-002
ADAMS:  
OFFICE         SRI:DRP/C   RI:DRP/C       SPE:DRP/C       ARI:DRP/C     C:DRS/EB2       D:DRP
Non-Publicly Available  
NAME             JSowa       BParks         CYoung       MOBanion         JDrake       AVegel
Non-Sensitive  
SIGNATURE         /RA/         /RA/           /RA/           /RA/           /RA/       /RA/
Keyword:
DATE           6/22/2018   6/21/2018       6/21/2018       6/25/2018     7/10/2018     7/18/18
By: CHY/RDR  
OFFICE         BC:DRP/C
Yes     No  
  NAME             JKozal
Publicly Available  
  SIGNATURE         /RA/
Sensitive
  DATE           7/18/18
NRC-002  
OFFICE  
SRI:DRP/C  
RI:DRP/C  
SPE:DRP/C  
ARI:DRP/C  
C:DRS/EB2  
D:DRP  
NAME  
JSowa  
BParks  
CYoung  
MOBanion  
JDrake  
AVegel  
SIGNATURE  
/RA/  
/RA/  
/RA/  
/RA/  
/RA/  
/RA/  
DATE  
6/22/2018  
6/21/2018  
6/21/2018  
6/25/2018  
7/10/2018  
7/18/18  
OFFICE  
BC:DRP/C  
   
NAME  
JKozal  
   
SIGNATURE  
/RA/  
   
DATE  
7/18/18
}}
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Latest revision as of 17:37, 5 January 2025

NRC Baseline Inspection Report 05000458/2018012
ML18194A413
Person / Time
Site: River Bend Entergy icon.png
Issue date: 07/18/2018
From: Jason Kozal
NRC/RGN-IV/DRP/RPB-C
To: Maguire W
Entergy Operations
Kozal J
References
IR 2018012
Download: ML18194A413 (32)


See also: IR 05000458/2018012

Text

July 18, 2018

Mr. William F. Maguire, Site Vice President

Entergy Operations, Inc.

River Bend Station

5485 U.S. Highway 61N

St. Francisville, LA 70775

SUBJECT:

RIVER BEND STATION - NRC BASELINE INSPECTION REPORT

05000458/2018012

Dear Mr. Maguire:

On July 16, 2018, the U.S. Nuclear Regulatory Commission (NRC) completed a baseline

inspection at your River Bend Station, Unit 1. On May 31 and July 16, 2018, the NRC

inspection team discussed the results of this inspection with you and other members of your

staff. The results of this inspection are documented in the enclosed report.

NRC inspectors documented five findings of very low safety significance (Green) in this report.

Four of these findings involved violations of NRC requirements. Additionally, NRC inspectors

documented two violations that were determined to be Severity Level IV under the traditional

enforcement process. The NRC is treating these violations as non-cited violations (NCVs)

consistent with Section 2.3.2.a of the NRC Enforcement Policy.

If you contest the violations or significance of these NCVs, you should provide a response within

30 days of the date of this inspection report, with the basis for your denial, to the U.S. Nuclear

Regulatory Commission, ATTN: Document Control Desk, Washington, DC 20555-0001; with

copies to the Regional Administrator, Region IV; the Director, Office of Enforcement; and the

NRC resident inspector at the River Bend Station.

If you disagree with a cross-cutting aspect assignment in this report, you should provide a

response within 30 days of the date of this inspection report, with the basis for your

disagreement, to the U.S. Nuclear Regulatory Commission, ATTN: Document Control Desk,

Washington, DC 20555-0001; with copies to the Regional Administrator, Region IV; and the

NRC resident inspector at the River Bend Station.

W. Maguire

2

This letter, its enclosure, and your response (if any) will be made available for public inspection

and copying at http://www.nrc.gov/reading-rm/adams.html and at the NRC Public Document

Room in accordance with 10 CFR 2.390, Public Inspections, Exemptions, Requests for

Withholding.

Sincerely,

/RA/

Jason W. Kozal, Chief

Project Branch C

Division of Reactor Projects

Docket No. 50-458

License No. NPF-47

Enclosure:

Inspection Report 05000458/2018012

w/ Attachment: Documents Reviewed

Enclosure

U.S. NUCLEAR REGULATORY COMMISSION

Inspection Report

Docket Number:

05000458

License Number:

NPF-47

Report Number:

05000458/2018012

Enterprise Identifier: I-2018-012-0015

Licensee:

Entergy Operations, Inc.

Facility:

River Bend Station

Location:

Saint Francisville, Louisiana

Inspection Dates:

February 1, 2018 to July 16, 2018.

Inspectors:

J. Sowa, Senior Resident Inspector

J. Drake, Senior Reactor Inspector

C. Young, Senior Project Engineer

M. OBanion, Resident Inspector (Acting)

B. Parks, Resident Inspector

Approved By:

J. Kozal, Chief, Branch C

Division of Reactor Projects

2

SUMMARY

The U.S. Nuclear Regulatory Commission (NRC) continued monitoring the licensees

performance by conducting a baseline inspection at River Bend Station in accordance with the

Reactor Oversight Process. The Reactor Oversight Process is the NRCs program for

overseeing the safe operation of commercial nuclear power reactors. Refer to

https://www.nrc.gov/reactors/operating/oversight.html for more information. Findings and

violations being considered in the NRCs assessment are summarized in the tables below.

List of Findings and Violations

Failure to Identify and Correct a Broken Feedwater Chemistry Probe

Cornerstone

Significance

Cross-cutting

Aspect

Report

Section

Barrier

Integrity

Green

NCV 05000458/2018012-02

Closed

None

71152 -

Problem

Identification

and

Resolution

Two examples of a self-revealed non-cited violation (NCV) of 10 CFR Part 50, Appendix B,

Criterion XVI, Corrective Action, were identified for the licensees failure to identify that a

broken chemistry probe in the feedwater system had the potential to cause an adverse impact

on plant safety, and promptly implement appropriate measures to address that condition.

Failure to Provide Adequate Procedures for Post-Scram Recovery

Cornerstone

Significance

Cross-cutting

Aspect

Report

Section

Mitigating

Systems

Green

NCV 05000458/2018012-06

Closed

None

71111.18 -

Plant

Modifications

The inspectors reviewed a self-revealed, non-cited violation of Technical Specification 5.4.1.a for

the licensees failure to establish, implement and maintain a procedure required by Regulatory

Guide 1.33, Revision 2, Appendix A, dated February 1978. Specifically, Procedure OSP-0053,

Emergency and Transient Response Support Procedure, Revision 22, which is required by

Regulatory Guide 1.33, inappropriately directed operations personnel to establish feedwater flow

to the reactor pressure vessel using the main feedwater regulating valve as part of the post-

scram actions. This resulted in the main feedwater regulating valves being operated outside

their design limits. This resulted in catastrophic failure of the main feedwater regulating valve

variseals and subsequent damage to multiple fuel assemblies.

3

Failure to Develop an Adequate Operational Decision-Making Issue for Compensatory Measures

Related to a Degraded Condition of the Feedwater System Sparger Nozzles

Cornerstone

Significance

Cross-cutting

Aspect

Report Section

Mitigating

Systems

Green

NCV 05000458/2018012-05

Closed

[H.9] -

Human

Performance,

Training

71111.15 -

Operability

Determinations

and

Functionality

Assessment

The inspectors identified a Green non-cited violation of 10 CFR Part 50, Appendix B, Criterion V,

Instructions, Procedures, and Drawings, for the failure to develop an adequate Operational

Decision-Making Issue (ODMI) document per Procedure EN-OP-111, Operational Decision-

Making Issue Process. Specifically, the licensee failed to develop an ODMI that provided

adequate guidance to the operators for safely operating the plant with degraded feedwater

sparger nozzles.

Failure to Establish Procedural Guidance for Determining Core Flow During Unanticipated

Single Loop Operations

Cornerstone

Significance

Cross-cutting

Aspect

Report

Section

Initiating

Events

Green

NCV 05000458/2018012-03

Closed

[P.3] -

Problem

Identification

and

Resolution,

Resolution

71153 -

Follow-up of

Events and

Notices of

Enforcement

Discretion

The inspectors reviewed a self-revealed, non-cited violation of 10 CFR Part 50 Appendix B,

Criterion V, Instructions, Procedures, and Drawings, for the licensees failure to establish

appropriate instructions in the abnormal operating procedure for thermal hydraulic instabilities.

Specifically, the procedural step for determining core flow when in single loop operations at low

power did not provide appropriate instructions to operators. As a result, station personnel could

not conclusively determine core flow and inserted a manual reactor scram.

Failure to Perform 10 CFR 50.59 Evaluation for Main Feedwater System Sparger Nozzle

Damage

Cornerstone

Significance

Cross-cutting

Aspect

Report

Section

None

SL-IV

NCV 05000458/2018012-07

Closed

None

71111.18 -

Plant

Modifications

The inspectors identified a Severity Level IV non-cited violation of 10 CFR 50.59, Changes,

Tests, and Experiments, for the licensees failure to provide a written safety evaluation for the

determination that operation with compensatory measures for damaged feedwater sparger

nozzles did not require a license amendment pursuant to 10 CFR 50.90, Application for

amendment of license, construction permit, or early site permit. Specifically, the licensee failed

to recognize that compensatory measures prohibiting operation in single loop conditions

required technical specification changes, and as such required prior NRC approval.

4

Failure to Conduct Adequate Transient Snap Shot Assessment Following Recirculation Pump

Trip

Cornerstone

Significance

Cross-cutting

Aspect

Report

Section

Initiating

Events

Green

FIN 05000458/2018012-01

Closed

None

71152 -

Problem

Identification

and

Resolution

The inspectors identified a finding for the licensees failure to adequately validate simulator

response during a transient snap shot assessment following an unexpected trip of reactor

recirculation pump A on December 19, 2012.

Failure to Submit a Licensee Event Report for a Manual Scram

Cornerstone

Significance

Cross-cutting

Aspect

Report

Section

None

SL-IV

NCV 05000458/2018012-04

Closed

None

71153 -

Follow-up of

Events and

Notices of

Enforcement

Discretion

The inspectors identified a Severity Level IV non-cited violation of 10 CFR 50.73, Licensee

Event Report System, for the licensees failure to submit a required licensee event report (LER).

Specifically, on February 1, 2018, after an unexpected trip of the recirculation pump B, the

licensee initiated a manual scram of the reactor that was not part of a preplanned sequence and

failed to submit an LER within 60 days.

5

INSPECTION SCOPES

Inspections were conducted using the appropriate portions of the inspection procedures (IPs) in

effect at the beginning of the inspection unless otherwise noted. Currently approved IPs with

their attached revision histories are located on the public website at http://www.nrc.gov/reading-

rm/doc-collections/insp-manual/inspection-procedure/index.html. Samples were declared

complete when the IP requirements most appropriate to the inspection activity were met

consistent with Inspection Manual Chapter (IMC) 2515, Light-Water Reactor Inspection

Program - Operations Phase. The inspectors reviewed selected procedures and records,

observed activities, and interviewed personnel to assess licensee performance and compliance

with Commission rules and regulations, license conditions, site procedures, and standards.

REACTOR SAFETY

71111.15Operability Determinations and Functionality Assessments (1 Sample)

The inspectors evaluated the following operability determinations and functionality

assessments:

(1) Review of Operational Decision-Making Issue (ODMI) associated with damaged

feedwater sparger on February 8, 2018

71111.18Plant Modifications (2 Samples)

The inspectors evaluated the following temporary or permanent modifications:

(1) OSP-0053, Emergency And Transient Response Support Procedure, following

decision to control reactor vessel level with main feedwater regulating valves during

post-scram operations

(2) Review of plant operation following modification to feedwater sparger nozzles 7 and 8

OTHER ACTIVITIES - BASELINE

71152Problem Identification and Resolution

Annual Follow-up of Selected Issues (3 Samples)

The inspectors reviewed the licensees implementation of its corrective action program

related to the following issues:

(1) Review of 1) simulator modelling of core parameters during a recirculation pump trip at

low power and 2) licensed operator training associated with single loop operations at low

power

(2) Actions to address a broken isokinetic chemistry sampling probe in the feedwater

system

(3) Actions to address fuel failures caused by debris material in the reactor vessel

6

71153Follow-up of Events and Notices of Enforcement Discretion

Personnel Performance (1 Sample)

(1) The inspectors evaluated operator response to the unexpected trip of the reactor

recirculation pump B on February 1, 2018.

INSPECTION RESULTS

Failure to Identify and Correct a Broken Feedwater System Chemistry Probe

Cornerstone

Significance

Cross-cutting

Aspect

Report

Section

Barrier

Integrity

Green

NCV 05000458/2018012-02

Closed

None

71152 -

Problem

Identification

and

Resolution

Two examples of a self-revealed Green finding and associated NCV of 10 CFR Part 50,

Appendix B, Criterion XVI, were identified for the licensees failure to identify that a broken

chemistry probe in the feedwater system had the potential to cause an adverse impact on

plant safety, and promptly implement appropriate measures to address that condition.

Description:

In 1999, the licensee initiated Condition Report CR-RBS-1999-1011 to document that an

isokinetic chemistry sample probe was found to be missing from its installed location in the

feedwater system, having broken off in the system. Following unsuccessful attempts to

locate and remove the missing probe, the licensee performed evaluation ER-99-0539 to

evaluate the potential impact of the missing probe on the continued operation and function of

feedwater system components. This evaluation concluded that the missing probe remaining

in the system would not present any hazard to any feedwater system components, and would

have no adverse effect on continued operation. This conclusion was based, in part, on a

calculation showing that feedwater flow would not have enough energy to levitate the probe

past a 20-foot vertical riser portion of the system, and therefore would not have the potential

to enter a feedwater sparger in the reactor vessel downstream of the vertical riser. Another

calculation showed that the impact energy of the loose probe on any feedwater components

would be negligible.

In March 2004, the NRC issued Information Notice (IN) 2004-06, Loss of Feedwater

Isokinetic Sampling Probes at Dresden Units 2 and 3 (ADAMS Accession No.

ML040711214). The IN discussed that broken probes had been discovered at five other

stations from 1990 to 2001, and further described the conditions discovered at Dresden

Nuclear Power Station (Dresden), Units 2 and 3. In 2003, three holes in a feedwater sparger

at Dresden Unit 2 were discovered, along with the missing feedwater probe in the sparger,

which had apparently caused the damage. Two probes were discovered to be in a feedwater

sparger in Dresden Unit 3, with no damage to the sparger having occurred yet. These

conditions demonstrated that not only could the probes be transported to the feedwater

spargers in the reactor vessel, but that they could potentially damage the spargers. The

licensees evaluation of this operating experience concluded that, since the broken probe at

River Bend had been replaced with a probe of a design not susceptible to the same failure,

no further action was needed. The licensee failed to address the potential impacts of the

adverse condition of the broken probe that remained loose in the feedwater system.

7

In 2011, the licensee documented an evaluation of a similar condition that had been

discovered at Brunswick Steam Electric Plant, Unit 2, where a feedwater sample probe was

discovered inside a feedwater sparger. The licensees evaluation of this operating

experience concluded that the current design (i.e. the probe that replaced the previous

broken probe) was not susceptible to this kind of failure. The licensee again failed to address

the impact of the previous broken probe that remained in the system, given that its potential

to be transported into a feedwater sparger in the reactor vessel had been shown.

In January 2018, the licensee discovered damage in the form of two holes in feedwater

sparger nozzles in the reactor vessel, with the broken probe protruding from one of the holes

in the direction of the other. The broken probe remaining in the feedwater system resulted in

potential adverse impacts on the reactor vessel wall due to impingement of feedwater flow

through the holes in the damaged sparger, as well as potential adverse impacts on the

integrity of fuel cladding due to the introduction of foreign material (pieces of the feedwater

sparger and chemistry probe) in the reactor vessel.

Corrective Actions: The broken probe was removed from the system. The licensee

performed evaluations to identify plant operational limitations to ensure that adverse impacts

to reactor pressure vessel wall integrity from additional holes in a feedwater sparger are

minimized. The licensee also issued an action to perform a review of historical loose parts

evaluations to add to tracking mechanisms and ensure adequacy of previous evaluations.

Corrective Action Reference: CR-RBS-2018-0294, CR-RBS-2018-0613, and

CR-RBS-2017-2828.

Performance Assessment:

Performance Deficiency: The licensees failure on two occasions to identify a broken

chemistry probe in the feedwater system had the potential to cause an adverse impact on

plant safety and to promptly implement appropriate measures to address that condition was a

performance deficiency.

Screening: The inspectors determined the performance deficiency was more than minor

because it was associated with the Cladding Performance, as well as the RCS Equipment

and Barrier Performance, attributes of the Barrier Integrity Cornerstone, and adversely

impacted the cornerstone objective to provide reasonable assurance that physical design

barriers (fuel cladding, reactor coolant system, and containment) protect the public from

radionuclide releases caused by accidents or events. Specifically, the unaddressed condition

of the broken probe remaining in the feedwater system resulted in damage to the feedwater

sparger, which resulted in thermal stresses to the reactor pressure vessel due to feedwater

impingement on the inner reactor pressure vessel wall, as well as the introduction of foreign

material inside the reactor vessel having the potential to result in damaged fuel. The licensee

performed an evaluation to determine what plant operational limitations were necessary in

order to ensure that additional thermal stresses on the reactor pressure vessel inner wall

remained below a threshold that would challenge the structural integrity of the vessel.

Significance: In accordance with Inspection Manual Chapter 0609, Appendix A, Section 5.0,

RCS boundary issues other than pressurized thermal shock are evaluated under the Initiating

Events Cornerstone. Using Inspection Manual Chapter 0609, Appendix A, The Significance

Determination Process for Findings At-Power, Exhibit 1, Initiating Events Screening

Questions, the finding was screened, as a potential loss of coolant accident (LOCA) initiator,

as having very low safety significance (Green) because, after a reasonable assessment of

8

degradation, the finding could not result in exceeding the RCS leak rate for a small LOCA and

could not have likely affected other systems used to mitigate a LOCA.

Cross-cutting Aspect: A cross-cutting aspect of P.5, Operating Experience, was determined

to be applicable to the performance deficiencies; however, no cross-cutting aspect was

assigned since the performance deficiencies occurred in 2004 and 2011, and are not

indicative of current licensee performance.

Enforcement:

Violation: Title 10 CFR Part 50, Appendix B, Criterion XVI, requires, in part, that measures

shall be established to assure that conditions adverse to quality, such as failures,

malfunctions, deficiencies, deviations, defective material and equipment, and

nonconformances are promptly identified and corrected. Contrary to the above, from

June 2004 to January 2018, the licensee failed to establish measures to assure that a

condition adverse to quality was promptly identified and corrected. Specifically, the licensee

failed to identify and correct a condition involving a broken sampling probe inside the

feedwater system. The uncorrected condition resulted in damage to a feedwater sparger,

with the potential to impact the available margin for integrity of the reactor vessel.

Disposition: This violation is being treated as a non-cited violation, consistent with

Section 2.3.2.a of the Enforcement Policy.

Failure to Provide Adequate Procedures for Post-Scram Recovery

Cornerstone

Significance

Cross-cutting

Aspect

Report

Section

Mitigating

Systems

Green

NCV 05000458/2018012-06

Closed

None

71111.18 -

Plant

Modifications

The inspectors reviewed a self-revealing, non-cited violation of Technical Specification 5.4.1.a

for the licensees failure to establish, implement and maintain a procedure required by

Regulatory Guide 1.33, Revision 2, Appendix A, dated February 1978. Specifically,

Procedure OSP-0053, Emergency and Transient Response Support Procedure,

Revision 22, which is required by Regulatory Guide 1.33, inappropriately directed operations

personnel to establish feedwater flow to the reactor pressure vessel using the main feedwater

regulating valve (MFRV) as part of the post-scram actions. This resulted in the MFRVs being

operated outside their design limits. This resulted in catastrophic failure of the MFRV

variseals and subsequent damage to multiple fuel assemblies.

Description:

In January 2015, the licensee revised Procedure OSP-0053, Emergency And Transient

Response Support Procedure, to use one of the three MFRVs to control reactor water level

following a scram event, and not use C33-LVF002, Start-Up FRV, which is designed to be

used for this application. This resulted in proceduralizing the use of a MFRV in circumstances

below the minimum controllable flow for the MFRV of 209,000 lbs/hr that the Main FRV

Copes Vulcan sizing datasheet provides as the a minimum controllable flow condition. As a

result of this change to the procedure to use a MFRV, the valves cycled numerous times in

the process of controlling level at low flow post-scram when feedwater flow demand was

below the MFRV minimum controllable flow volume. This repeated cycling of the valve led to

excessive open/close cycling of the MFRVs and caused the catastrophic failure of the

variseals.

9

As a result, foreign material parts of the variseal were introduced into the core. It is

suspected that this material resulted in six nuclear fuel cladding failures caused by debris

fretting.

Corrective Actions: The licensee revised Procedure OSP-0053, Emergency and Transient

Response Support Procedure, to control reactor vessel level post scram using a startup

feedwater regulating valve and modified the design of the MFRV variseal.

Corrective Action Reference: CR-RBS-2016-00893

Performance Assessment:

Performance Deficiency: The failure to establish adequate procedural guidance for operation

of the main feedwater system was a performance deficiency.

Screening: The performance deficiency was more than minor, and therefore a finding,

because it was associated with the procedure quality attribute of the Mitigating Systems

Cornerstone and adversely affected the cornerstone objective to ensure the availability,

reliability, and capability of systems that respond to initiating events to prevent undesirable

consequences. Specifically, Procedure OSP-0053, Emergency and Transient Response

Support Procedure, Revision 22, inappropriately directed operations personnel to establish

feedwater flow to the reactor pressure vessel using the MFRV as part of the post-scram

actions. This resulted in the MFRVs being operated outside their design limits.

Significance: The inspectors screened the finding in accordance with Inspection Manual

Chapter 0609, Appendix A, The Significance Determination Process for (SDP) for Findings

At-Power. Using Inspection Manual Chapter 0609, Appendix A, Exhibit 2, Mitigating

Systems Screening Questions, the inspectors determined this finding was of very low safety

significance (Green) because the finding: (1) was not a deficiency affecting the design or

qualification of a mitigating structure, system, or component, and did not result in a loss of

operability or functionality; (2) did not represent a loss of system and/or function; (3) did not

represent an actual loss of function of at least a single train for longer than its technical

specification allowed outage time, or two separate safety systems out-of-service for longer

than their technical specification allowed outage time; and (4) did not represent an actual loss

of function of one or more nontechnical specification trains of equipment designated as high

safety-significant in accordance with the licensees maintenance rule program.

Cross-cutting Aspect: No cross-cutting aspect was assigned since the performance

deficiency occurred in January 2015 and is not indicative of current licensee performance.

Enforcement:

Violation: Technical Specification 5.4.1.a requires in part, that written procedures shall be

established, implemented, and maintained covering the applicable procedures recommended

in Regulatory Guide 1.33, Revision 2, Appendix A, dated February 1978. Regulatory

Guide 1.33, Appendix A, Section 6.u., identifies procedures for responding to a reactor trip as

required procedures. Procedure OSP-0053, Attachment 16, Post Scram

Feedwater/Condensate Manipulations Below 5% Reactor Power, was a procedure

established by the licensee for responding to a reactor trip.

Contrary to the above, from January 30, 2015, until April 13, 2017, the licensee failed to

maintain adequate written procedures for responding to a reactor trip. Specifically,

Procedure OSP-0053 inappropriately directed operations personnel to establish feedwater

10

flow to the reactor pressure vessel using the MFRV as part of the post-scram actions. The

MFRV operator characteristics are not designed to operate at the low flow conditions

immediately following a reactor scram from high power. As a result, the MFRV variseals

degraded and resulted in damage to multiple fuel assemblies. Subsequent to the event, the

licensee changed the procedure, directing operations personnel to utilize one of the startup

feedwater regulating valves.

Disposition: This violation is being treated as an non-cited violation consistent with

Section 2.3.2.a of the NRC Enforcement Policy.

Failure to Develop an Adequate Operational Decision-Making Issue for Compensatory

Measures Related to a Degraded Condition of the Feedwater System Sparger Nozzles

Cornerstone

Significance

Cross-cutting

Aspect

Report Section

Mitigating

Systems

Green

NCV 05000458/2018012-05

Closed

[H.9] -

Human

Performance,

Training

71111.15 -

Operability

Determinations

and

Functionality

Assessments

The inspectors identified a Green non-cited violation of 10 CFR Part 50, Appendix B,

Criterion V, Instructions, Procedures, and Drawings, for the failure to develop an adequate

operational decision-making issue (ODMI) document per Procedure EN-OP-111, Operational

Decision-Making Issue Process. Specifically, the licensee failed to develop an ODMI that

provided adequate guidance to the operators for safely operating the plant with degraded

feedwater sparger nozzles.

Description:

During a reactor startup on February 1, 2018, reactor recirculation pump B unexpectedly

tripped during an attempted upshift to fast speed. As a result, the plant was operating with

recirculation pump A in fast speed and recirculation pump B not running. Prior to this startup,

during an outage that was being conducted to replace failed fuel assemblies, damage to

feedwater sparger nozzles was identified.

Example 1: The evaluation of the damaged feedwater sparger nozzles 7 and 8 on

sparger N4C identified that the damaged sections of the feedwater sparger nozzles had the

potential to adversely affect the vessel cladding by allowing relatively colder water to directly

flow into the relatively hotter vessel wall, thus inducing thermal fatigue. All components of the

reactor coolant system (RCS) are designed to withstand effects of cyclic loads due to system

pressure and temperature changes. These loads are introduced by startup (heatup) and

shutdown (cooldown) operations, power transients, and reactor trips. Limits are established

for pressure and temperature changes during RCS heatup and cooldown, such that plant

systems remain within the design assumptions and the stress limits for cyclic operation.

Limits on RCS pressure, temperature, heatup rate, and cooldown rate define allowable

operating regions and operating cycles to prevent nonductile failure of system components.

Because operation with the sparger nozzle damage was outside the limits originally analyzed,

the licensee requested General Electric-Hitachi (GEH) to provide an operability analysis of

the degraded condition. GEH Report 004N6557, Revision 0, dated January 26, 2018,

Operability Assessment of the River Bend Station Feedwater Sparger Assembly in the

January 2018 As-found Condition, stated, in part, this evaluation does not account for Final

11

Feedwater Temperature Reduction (FFWTR), Feedwater Heater Out-of-Service (FWH OOS)

conditions, nor Single Loop Operation (SLO) operating conditions. Based on this analysis,

the licensees engineering department concluded that the recommended classification of this

condition was OPERABLE-COMP MEAS (operable with compensatory measures), with the

degraded/nonconforming condition being the holes in the feedwater sparger nozzles. Based

on the results of this analysis, one of the operational restrictions/limitations stipulated in the

licensees ODMI was that, RBS will not operate in Single Loop Operation (SLO).

The ODMI developed by the licensee included two trigger points:

Trigger Point 1:

An unexpected operational state below approximately 85 percent power in which the vessel

wall-to-feedwater delta-T stabilizes at less than or equal to 154 degrees Fahrenheit (F), as

detected by periodic monitoring during normal operations, OR due to a transient as defined

above.

Trigger Point 2:

An unexpected operational state in which the vessel wall-to-feedwater delta-T stabilizes at

greater than 154 degrees F, as detected by periodic monitoring during normal operations, OR

due to a transient as defined above.

The ODMI failed to provide adequate guidance to the operators if they found themselves in

any of the conditions that GEH had listed as not being evaluated for continued operation with

the degraded condition. When reactor recirculation pump B failed to shift to fast speed at

9:46 a.m., the operators logged entry into Procedure GOP-004, Single Loop Operations.

The plant was in single loop operating conditions, and remained there until 10:57 a.m. when

the Mode switch was placed in shutdown. The ODMI failed to provide adequate guidance on

the actions required if the plant entered any of the conditions that were not evaluated for the

degraded sparger condition. In addition, the Just In Time Training given to the operators

prior to taking the watch to commence power operations with the degraded condition did not

address these issues either. As a result, rather than take prompt actions to place the plant in

a known safe condition upon entry into single loop operations, the control room supervisor

requested that GEH be contacted to determine if it was acceptable to remain in single loop

operations.

Example 2: The evaluation of the damaged feedwater sparger nozzles 7 and 8 on

sparger N4C identified that the damaged sections of the feedwater sparger nozzles had the

potential to adversely affect the B narrow range level instrument. The damage on feedwater

sparger N4C created unexpected feedwater flow paths in the reactor vessel during plant

operation that had the potential to adversely affect the "B" variable leg reactor water level

instruments. There were two potential impacts of this condition on indicated level from

narrow range level instruments that tap off of the B variable leg. Flow from the holes in the

feedwater sparger nozzle elbows could flow across the variable leg nozzle opening at AZ

200 degrees (B Leg), lowering the pressure on the variable leg side of the differential

pressure measurements, or the flow from the sparger nozzle damage could directly impact

the B variable leg, increasing the pressure on the variable leg side of the differential pressure

measurements.

12

The narrow range RPV level instrumentation supports two reactor water level trips: low level

(Level 3) and high level (Level 8). During a transient or accident event where the RPV water

level is changing, the trip signal from the B narrow range instrument could be affected.

Based on the GE report, during a transient or accident event where the RPV water level is

increasing, the high level (Level 8) trips (RPS trip and Feedwater Pump trip) in the affected

channel may occur later than the trips in the unaffected channels. This may delay the overall

Level 8 trips. For the Level 8 RPS trip, the margin between the calculated nominal trip

setpoint and the technical specification allowable value is 0.77 inches. For the Level 3 RPS

trip, the margin between the calculated nominal trip setpoint and the technical specification

allowable value is 0.67 inches. An operability determination of the narrow range level

instruments was performed under CR-RBS-2018-00633 CA-01.

The ODMI developed by the licensee included two trigger points:

Trigger Point 1:

Action: Refer to applicable SRs as specified by STP-000-0001, Att. 9.2

Step 30 in STP-000-0001 not within 4 inches

Step 71 in STP-000-0001 not within 6 inches

Notify the Duty Manager and the Ops Duty Manager

Trigger Point 2:

The magnitude of the B channel deviation is 1.5 inches in either direction from the average

of the A, C and D channel average + 1.1 inches.

Notify the Duty Manager and the Engineering Duty Manager.

The ODMI implemented by the licensee allowed level indication deviation in the affected

channel for the B21-LTN080 instruments to be monitored to ensure it remained within the

allowable margin to ensure the technical specification trip limit is not exceeded. It stated in

part that, If the deviation exceeds a change of 1.5 inches from historical deviation of

1.1 inches above the average of the A, C, and D channels in either an increasing or

decreasing direction, then condition will be evaluated by engineering. The monitored trigger

point of +1.5 inches will provide adequate margin for both the Level 3 and Level 8 trips.

However, if a 1.5-inch bias in the low direction would have been reached, two Technical

Specification (TS) Allowable Values could have been exceeded (by 0.5 inches for TS

Table 3.3.5.2-1, Function 2, Reactor Core Isolation Cooling System Instrumentation, and by

0.49 inches for TS Table 3.3.5.2-1, Function 5, Reactor Protection System Instrumentation).

The 1.5-inch bias in the low direction would have rendered the instrument inoperable based

on 10 CFR 50.36(c)(2)(i), which states, Limiting conditions for operation are the lowest

functional capability or performance levels of equipment required for safe operation of the

facility. Since the limiting conditions for operations (LCOs) include Allowable Values (e.g.,

LCO 3.3.5.2 includes Table 3.3.5.2-1 which has Allowable Values for Functions 2 and 5), the

Allowable Values are understood to be the lowest functional capability or performance levels

of equipment required for safe operation of the facility.

The licensees technical specifications provide the following guidance: Surveillance

Requirement 3.0.1, Failure to meet a Surveillance, whether such failure is experienced

during the performance of the Surveillance or between performances of the Surveillance,

shall be failure to meet the LCO.

13

1.1 Definitions: A CHANNEL CALIBRATION shall be the adjustment, as necessary, of the

channel output such that it responds within the necessary range and accuracy to known

values of the parameter that the channel monitors

In addition, the TS Bases state, SR 3.0.1 through SR 3.0.4 establish the general

requirements applicable to all Specifications and apply at all times, unless otherwise stated.

The OPERABILITY of the RPS (Reactor Protection System) is dependent on the

OPERABILITY of the individual instrumentation channel Functions specified in

Table 3.3.1.1-1. Each Function must have a required number of OPERABLE channels [2 per

RPS trip system for the vessel level function] per RPS trip system, with their setpoints within

the specified Allowable Value, where appropriate. The actual setpoint is calibrated consistent

with applicable setpoint methodology assumptions. Each channel must also respond within

its assumed response time. Allowable Values are specified for each RPS Function specified

in the Table. Nominal trip setpoints are specified in the setpoint calculations. The nominal

setpoints are selected to ensure that the actual setpoints do not exceed the Allowable Value

between successive channel calibrations. Operation with a trip setpoint less conservative

than the nominal trip setpoint, but within its Allowable Value, is acceptable. A channel is

inoperable if its actual trip setpoint is not within its required Allowable Value.

Process effects impact the establishment of the appropriate Nominal Trip Setpoint, which is

determined by addressing all instrument channel uncertainties (including biases) and

offsetting them from the Analytical Limit. The currently licensed Allowable Values are fixed

within the technical specification tables. Nominal Trip Setpoints are established on the basis

of a calculation that identifies all known uncertainties between the Analytical Limit and the

Nominal Trip Setpoint. If a new, unaccounted-for process effect bias in the nonconservative

direction is discovered, this effect needs to be reflected in the calculation of a new Nominal

Trip Setpoint and a corresponding new Allowable Value. However, in this case, the licensee

did not elect to pursue a license amendment or other process to change its currently licensed

Allowable Value, nor did it ask for a temporary enforcement discretion. Therefore, with the

new (unaccounted for) postulated process effect present, this has the effect of making the

existing Nominal Trip Setpoint (calibrated value) offset in the nonconservative direction by the

amount of the new postulated process effect (i.e., up to 1.5 inches), which reduces the margin

between the actual trip setpoint and the existing licensed Allowable Value.

Therefore, to meet the River Bend technical specification requirement that a channel be

considered inoperable if its actual trip setpoint is not within its required Allowable Value

without changing the currently licensed Allowable Value, only approximately a 1/2-inch of the

1.5 inches of new postulated process effect can be accommodated between the existing

calibrated setpoint and the (existing) licensed Allowable Value. Thus, the direction to notify

engineering only if the Rx vessel level indication bias had reached a value of 1.5 inches in

either direction was inadequate direction for the operating staff in order to ensure that the

instruments remained operable.

Corrective Actions: The licensee corrected the condition by revising the ODMI to include

adequate operator guidance and trigger points.

Corrective Action Reference: CR-RBS-2018-03148

14

Performance Assessment:

Performance Deficiency: The failure to establish ODMI guidance per Procedure EN-OP-111

to address the compensatory measures implemented to maintain operability of the plant with

degraded feedwater sparger nozzles was a performance deficiency.

Screening: For Example 1, the performance deficiency was more than minor, and therefore a

finding, because it was associated with the equipment reliability attribute of the Mitigating

Systems Cornerstone and adversely affected the cornerstone objective to ensure the

availability, reliability, and capability of systems that respond to initiating events to prevent

undesirable consequences. Specifically, the licensee failed to provide adequate guidance to

the operators for actions required if the plant inadvertently entered any of the unanalyzed

conditions for continued operation with the degraded sparger. For Example 2, the

performance deficiency was more than minor, and therefore a finding, because if left

uncorrected it would have the potential to lead to a more significant safety concern.

Specifically, the use of less conservative calculated values than the Allowable Values stated

in the facility TS as a basis for establishing a threshold for operability of TS equipment could

result in the inappropriate evaluation of actual degraded conditions that impact the ability of

components to perform their required safety functions.

Significance: The inspectors screened the finding in accordance with Inspection Manual

Chapter 0609, Appendix A, The Significance Determination Process for (SDP) for Findings

At-Power. Using Inspection Manual Chapter 0609, Appendix A, Exhibit 1, Initiating Events

Screening Questions, the inspectors determined this finding was of very low safety

significance (Green) because for Example 1, the finding would not result in exceeding the

RCS leak rate for a small LOCA and could not have likely affected other systems used to

mitigate a LOCA. For Example 2, it was not a design/qualification deficiency, did not

represent a loss of system safety function, did not result in a loss of function of a single train

for greater than its TS-allowable outage time, did not result in a loss of function of nonsafety-

related risk-significant equipment and was not risk significant due to external events. In

addition, no actual deviation of the B narrow range level instrument was observed during

plant startup on February 9, 2018.

Cross-cutting Aspect: This finding had a cross-cutting aspect of human performance, change

management H.3: Leaders use a systematic process for evaluating and implementing

change so that nuclear safety remains the overriding priority. Specifically, the licensee did

not use a systematic process to develop and verify the adequacy of the ODMIs associated

with the compensatory measures implemented for the degraded sparger.

Enforcement:

Violation: Title 10 CFR Part 50, Appendix B, Criterion V, requires in part that, activities

affecting quality shall be prescribed by documented instructions, procedures, or drawings, of

a type appropriate to the circumstances. Licensee Procedure EN-OP-111, Operational

Decision-Making Issue (ODMI) Process, Revision 16, an Appendix B quality-related

procedure, provides instructions for developing guidance for plant operation with

compensatory measures in place to maintain plant system operable with degraded

conditions. Procedure EN-OP-111, step 5.2.4, states that Operational Decision-Making

Considerations should ensure that a course of action is selected based upon a critical

consideration of risks and potential consequences, as well as a thorough understanding of

alternate solutions. The final decision should be a deliberate act, providing clear direction,

trigger points, contingencies, and abort criteria. The Action Plans should provide clear

15

guidance in each ODMI which delineate actions to be taken when conditions escalate

unexpectedly, conditions are outside the scope of the ODMI analysis, or actions are not able

to be implemented. Actions that contain recommendations to "consider or evaluate" in

response to triggers should be avoided. When such actions are used, a definite period to

finish the evaluation or consideration should be provided.

Contrary to the above, prior to February 1, 2018, the licensee failed to ensure that the ODMIs

provided a course of action based upon a critical consideration of risks and potential

consequences, as well as a thorough understanding of alternate solutions; and that the final

decision was a deliberate act providing clear direction, trigger points, contingencies, and abort

criteria. Specifically, the licensee failed to develop adequate guidance for the operators to

maintain safe operation of the plant with compensatory measures in place for degraded

feedwater sparger nozzles. The action plans failed to provide clear guidance in each ODMI

to delineate actions to be taken when conditions escalate unexpectedly; instead, the actions

specified directed the operators to consult with offsite contractors regarding the acceptability

of allowing the plant to remain in operation with given conditions.

Disposition: This violation is being treated as a non-cited violation, consistent with

Section 2.3.2.a of the NRC Enforcement Policy.

Failure to Establish Procedural Guidance for Determining Core Flow During Unanticipated

Single Loop Operations

Cornerstone

Significance

Cross-cutting

Aspect

Report

Section

Initiating

Events

Green

NCV 05000458/2018012-03

Closed

[P.3] -

Problem

Identification

and

Resolution,

Resolution

71153 -

Follow-up of

Events and

Notices of

Enforcement

Discretion

The inspectors reviewed a self-revealed, non-cited violation of 10 CFR Part 50, Appendix B,

Criterion V, Instructions, Procedures and Drawings, for the licensees failure to establish

appropriate instructions in the abnormal operating procedure for thermal hydraulic

instabilities. Specifically, the procedural step for determining core flow when in single loop

operations at low power did not provide appropriate instructions to operators. As a result,

station personnel could not conclusively determine core flow and inserted a manual reactor scram.

Description:

On February 1, 2018, with the unit in Mode 1 at approximately 27 percent power, reactor

recirculation pump B unexpectedly tripped during an upshift in the speed of the pump. As a

result, the reactor was in a single loop configuration with the recirculation pump A running in

fast speed and the recirculation pump B not running. Operators entered Abnormal Operating

Procedure AOP-0024, Thermal Hydraulic Instability Controls, Revision 30, as a result of the

unplanned entry into single loop operations. Step 5.8 of this procedure directed operators to

determine core flow and enter the General Operating Procedure GOP-004, for single loop

operations. Step 5.8 also instructed operators to determine core flow using process computer

point B33NA01V when in a configuration with one recirculation pump in fast speed and one

recirculation pump off. Control room operators observed the value of this data point as

13.9 Mlbm/hr. The operators concluded that this value was not valid since the indicated flow

16

was much lower than expected with one recirculation pump running in fast speed. The

operators then observed a value of 27.3 Mlbm/hr core flow using the ERIS data point for

B33NA01V. This value appeared to be a valid number based on the single loop operation

power/flow map contained in AOP-0024, Attachment 2. Normal data points are displayed in

ERIS with a white text, but control room operators observed the ERIS data point displayed in

a magenta color. Additionally, the word suspect appeared adjacent to the data point for

core flow. Control room operators contacted information technology personnel and attempted

to understand the magenta color and suspect information associated with the core flow data

point. Concurrently, operators attempted to validate core flow using alternate means but

were unsuccessful as the alternate indications did not provide accurate core flow readings at

low reactor power when in a single loop configuration. After approximately one hour spent

seeking to understand the unfamiliar indication associated with B33NA01V, control room

operators conducted a brief and made the decision to shut down the unit due to the

uncertainties associated with the core flow data point. Following plant shutdown and

subsequent troubleshooting and investigation, licensee personnel concluded that the

magenta text and suspect note associated with ERIS B33NA01V was an expected system

response. Below approximately 40 percent core flow, the plant process computer shifts the

calculation method from the primary means of calculating core flow using the sum of jet pump

flows to an alternate process that uses core plate differential pressure. As a result of shifting

to the alternate calculation of core flow, data point ERIS B33NA01V was programmed to turn

magenta in color and display suspect to alert operators that the method of calculating core

flow had changed.

The inspectors reviewed Condition Report CR-RBS-2012-07759. This condition report was

generated by operations department personnel on December 19, 2012, and identified that

ERIS point B33NA01V indicated suspect and was not available for use. The condition

report also stated that this data point was needed for determining core flow when the plant

configuration consisted of one recirculation pump running in fast speed and another

recirculation pump was off. The inspectors confirmed that this condition report was generated

during a single loop plant configuration that was the result of an unanticipated reactor

recirculation pump A trip on December 19, 2012. The condition report corrective actions

explained the reason for the suspect reading of ERIS point B33NA01V. No corrective

actions were generated to address AOP-0024, which directs licensed operators to validate

core flow in single loop operations. Additionally, no corrective actions were generated to

validate plant simulator response to unanticipated single loop operations.

Corrective Actions: After this information was disseminated to licensed operators, the

licensee implemented procedural changes to AOP-0024 that provided amplifying information

regarding B33NA01V validated core flow. Specifically, the licensee revised the procedure on

February 7, 2018, in order to 1) direct operators to determine core flow using ERIS data point

B33NA01V during single loop operations when core flow is below 40 percent and 2) provide

clear guidance regarding expected system response of the process computer data points

during abnormal flow configurations.

Corrective Action Reference: CR-RBS-2018-00776

Performance Assessment:

Performance Deficiency: The failure to establish appropriate guidance to determine core flow

during single loop operations in quality-related abnormal operating procedure AOP-0024,

Thermal Hydraulic Instability Controls, Revision 30, was a performance deficiency.

17

Screening: The performance deficiency was more than minor, and therefore a finding,

because it was associated with the procedure quality attribute of the Initiating Events

Cornerstone and adversely affected the cornerstone objective to limit the likelihood of events

that upset plant stability. Specifically, the failure to understand core flow data indicated by

plant process computer point B33NA01V and ERIS data point B33NA01V resulted in

confusion and the ultimate decision to insert a manual reactor scram.

Significance: The inspectors screened the finding in accordance with Inspection Manual

Chapter 0609, Appendix A, The Significance Determination Process for (SDP) for Findings

At-Power. Using Inspection Manual Chapter 0609, Appendix A, Exhibit 1, Initiating Events

Screening Questions, the inspectors determined this finding is of very low safety significance

(Green) because the finding did not cause a reactor trip and the loss of mitigation equipment

relied upon to transition the plant from the onset of the trip to a stable shutdown condition.

Cross-cutting Aspect: This finding has a cross-cutting aspect in the area of problem

identification and resolution, resolution, because the licensee failed to take effective

corrective actions to address issues in a timely manner commensurate with their safety

significance. Specifically, the station failed to implement procedure changes to AOP-0024

after discovering similar confusing indications associated with B33NA01V on

December 19, 2012.

Enforcement:

Violation: Title 10 CFR Part 50, Appendix B, Criterion V, requires in part that, activities

affecting quality shall be prescribed by documented instructions, procedures, or drawings, of

a type appropriate to the circumstances.

Contrary to the above, prior to February 7, 2018, the licensee failed to provide a procedure of

a type appropriate to the circumstances for an activity affecting quality. Specifically,

AOP-0024, Thermal Hydraulic Stability Controls, a quality-related procedure, was not

appropriate to the circumstances. AOP-0024 did not provide accurate and adequate

instruction to operators to determine core flow during single loop operations. The licensee

restored compliance by revising AOP-0024 to include accurate and adequate guidance to

determine core flow during unanticipated single loop operations.

Disposition: This violation is being treated as an non-cited violation consistent with

Section 2.3.2.a of the NRC Enforcement Policy.

Failure to Perform 10 CFR 50.59 Evaluation for Main Feedwater System Sparger Nozzle

Damage

Cornerstone

Significance

Cross-cutting

Aspect

Report

Section

None

SL-IV

NCV 05000458/2018012-07

Closed

None

71111.18 -

Plant

Modifications

The inspectors identified a Severity Level IV NCV of 10 CFR 50.59, Changes, Tests, and

Experiments, for the licensees failure to provide a written safety evaluation for the

determination that operation with compensatory measures for damaged feedwater sparger

nozzles did not require a license amendment pursuant to 10 CFR 50.90, Application for

amendment of license, construction permit, or early site permit. Specifically, the licensee

18

failed to recognize that compensatory measures prohibiting operation in single loop

conditions were technical specification changes, and as such required prior NRC approval.

Description:

During an outage that was conducted to replace failed fuel assemblies in January 2018,

damage to feedwater sparger nozzles was identified. The evaluation of the damaged

feedwater sparger nozzles #7 and #8 on sparger N4C identified that the damaged sections of

the feedwater sparger nozzles had the potential to adversely affect the vessel cladding by

allowing relatively colder water to directly flow into the relatively hotter vessel wall, thus

inducing thermal fatigue. All components of the RCS are designed to withstand effects of

cyclic loads due to system pressure and temperature changes. These loads are introduced

by startup (heatup) and shutdown (cooldown) operations, power transients, and reactor trips.

Limits are established for pressure and temperature changes during RCS heatup and

cooldown, such that plant systems remain within the design assumptions and the stress limits

for cyclic operation. Limits on RCS pressure, temperature, heatup rate, and cooldown rate

define allowable operating regions and operating cycles to prevent nonductile failure of

system components. Because operation with the sparger nozzle damage was outside the

limits originally analyzed, the licensee requested General Electric-Hitachi (GEH) to provide an

operability analysis of the degraded condition. GEH Report #004N6557 Revision 0, dated

January 26, 2018, Operability Assessment of the River Bend Station Feedwater Sparger

Assembly in the January 2018 As-found Condition, stated in part, this evaluation does not

account for Final Feedwater Temperature Reduction (FFWTR), Feedwater Heater Out-of-

Service (FWH OOS) conditions, nor Single Loop Operation (SLO) operating conditions.

Based on this analysis, the licensees engineering department concluded that the

recommended classification of this condition was OPERABLE-COMP MEAS (operable with

compensatory measures), with the degraded/nonconforming condition being the holes in the

feedwater sparger nozzles. One of the operational restrictions/limitations was that, RBS will

not operate in Single Loop Operation (SLO). These compensatory measures directly

affected Technical Specification (TS) 3.4.1, Recirculation Loops Operating. The TS limiting

condition for operation (LCO) B, One recirculation loop shall be in operation, which is

applicable when operating in Modes 1 and 2, had the following limitations:

1.

THERMAL POWER 77.6% rated thermal power (RTP);

2.

Total core flow within limits;

3.

LCO 3.2.1,"AVERAGE PLANAR LINEAR HEAT GENERATION RATE (APLHGR),"

single loop operation limits specified in the Core Operating Limits Reports (COLR);

4.

LCO 3.2.2,"MINIMUM CRITICAL POWER RATIO (MCPR)," single loop operation

limits specified in the COLR; and

5.

LCO 3.3.1.1, "Reactor Protection System (RPS) Instrumentation," Function 2.b

(Average Power Range Monitors Flow Biased Simulated Thermal Power- High), Allowable

Value for single loop operation as specified in the COLR.

The licensees compensatory measures established a more restrictive LCO whereby Single

Loop Operations are limited by more restrictive criteria than those stated in the existing LCO.

Specifically, the licensees compensatory measures stated that the station would not operate

in Single Loop Operation.

NRC Administrative Letter 98-10: Dispositioning of Technical Specifications That Are

Insufficient To Assure Plant Safety, dated December 29, 1988, provides the following

guidance:

19

Title 10 of the Code of Federal Regulations, Section 50.36, Technical Specifications

requires that each TS limiting condition for operation (LCO) specify, at a minimum, the lowest

functional capability or performance level of equipment required for the safe operation of the

facility.

IMC0326 states, in part: Additionally, if a compensatory measure involves a temporary facility

or procedure change, 10 CFR 50.59 should be applied to the temporary change with the

intent to determine whether the temporary change/compensatory measure itself (not the

degraded or nonconforming condition) impacts other aspects of the facility or procedures

described in the UFSAR. In considering whether a temporary facility or procedure change

impacts other aspects of the facility, a licensee should apply 10 CFR 50.59, paying particular

attention to ancillary aspects of the temporary change that result from actions taken to directly

compensate for the degraded condition. Whenever degraded or nonconforming conditions

are discovered, 10 CFR Part 50, Appendix B, requires prompt corrective action to correct or

resolve the condition.

In summary, the discovery of an improper or inadequate TS value or required action is

considered a degraded or nonconforming condition as defined in IMC0326. Imposing

administrative controls in response to an improper or inadequate TS is considered an

acceptable short-term corrective action. The NRC staff expects that, following the imposition

of administrative controls, an amendment to the TS, with appropriate justification and

schedule, will be submitted in a timely fashion. Once any amendment correcting the TS is

approved, the licensee must update the final safety analysis report, as necessary, to comply

with 10 CFR 50.71(e).

Because the licensee did not perform a 50.59 screening for the compensatory measures

associated with the restricted operating conditions, the licensee failed to recognize that the

TSs were now non-conservative and that NRC approval was required.

Corrective Actions: The licensee documented the violation in the corrective action program

and created actions to review 50.59 screening requirements.

Corrective Action Reference: CR-RBS-2018-03147

Performance Assessment:

Performance Deficiency: The failure to perform a written safety evaluation for the effect of

compensatory measures implemented due to degraded feedwater sparger nozzles was a

performance deficiency.

Screening: The performance deficiency was evaluated in accordance with the traditional

enforcement process because it impacted the ability of the NRC to perform its regulatory

oversight function.

Significance: Using example 6.1.d.2 from the NRC Enforcement Policy, the violation was

determined to be a Severity Level IV violation.

Cross-cutting Aspect: Because the violation was dispositioned using the traditional

enforcement process, no cross cutting aspect was assigned.

20

Enforcement:

Violation: Title 10 CFR 50.59(d)(1) requires, in part, that the licensee shall maintain records

of changes in the facility, of changes in procedures, and of tests and experiments as

described in the updated final safety analysis report (UFSAR). These records must include a

written evaluation which provides a basis for the determination that the change, test, or

experiment does not require a license amendment.

Contrary to the above, since January 29, 2018, the licensee failed to maintain records of a

change to the facility, as described in the UFSAR, that include a written evaluation which

provides a basis for the determination that the change did not require a license amendment.

Specifically, the licensee made changes pursuant to 10 CFR 50.59(c) to the plant as

described in the UFSAR and did not provide a written evaluation for the determination that

compensatory measures prohibiting operation in single loop condition were technical

specification changes, and as such required prior NRC approval.

Disposition: This violation is being treated as an non-cited violation consistent with

Section 2.3.2.a of the NRC Enforcement Policy.

Failure to Conduct Adequate Transient Snap Shot Assessment Following Recirculation Pump

Trip

Cornerstone

Significance

Cross-cutting

Aspect

Report

Section

Initiating Events

Green

FIN 05000458/2018012-01

Closed

None

71152 -

Problem

Identification

and

Resolution

The inspectors identified a Green finding for the licensees failure to adequately validate

simulator response during a transient snap shot assessment following an unexpected trip of

reactor recirculation pump A on December 19, 2012.

Description:

On December 19, 2012, with the plant operating at 100 percent power, reactor recirculation

pump A unexpectedly tripped off. As a result, the plant configuration consisted of one

recirculation pump running in fast speed and the other recirculation pump secured. During

this single loop configuration, station personnel identified that emergency response

information system (ERIS) point B33NA01V indicated suspect and was not available for

use. The station documented this condition in Condition Report CR-RBS-2012-07759.

On February 1, 2018, with the unit in Mode 1 at approximately 27 percent power, reactor

recirculation pump B unexpectedly tripped during an upshift in the speed of the pump. As a

result, the reactor was in a single loop configuration with the recirculation pump A running in

fast speed and the recirculation pump B not running. Operators entered abnormal operating

procedure AOP-0024, Thermal Hydraulic Instability Controls, Revision 30, as a result of the

unplanned entry into single loop operations. Step 5.8 of this procedure directed operators to

determine core flow and enter general operating procedure GOP-004, Single Loop

Operations. Step 5.8 also instructed operators to determine core flow using process

computer point B33NA01V (which can be observed in both ERIS and the plant process

computer) when in a configuration with one recirculation pump in fast speed and one

21

recirculation pump off. Control room operators observed the value of this data point as

13.9 million pounds mass per hour (Mlbm/hr) of flow through the reactor core. The operators

concluded that this value was not valid since the indicated flow was much lower than

expected with one recirculation pump running in fast speed. The operators then observed a

value of 27.3Mlbm/hr core flow using the ERIS data point for B33NA01V. This value

appeared to be a valid number based on the single loop operation power/flow map contained

in AOP-0024, Attachment 2. Normal data points on ERIS are displayed with a white text, but

control room operators observed the ERIS data point displayed in a magenta color.

Additionally, the word suspect appeared adjacent to the data point for core flow. Control

room operators contacted information technology personnel and attempted to understand the

magenta color and suspect information associated with the core flow data point.

Concurrently, operators attempted to validate core flow using alternate means but were

unsuccessful, as the alternate indications did not provide accurate core flow readings at low

reactor power when in a single loop configuration. After approximately one hour spent

seeking to understand the unfamiliar indication associated with B33NA01V, control room

operators conducted a brief and made the decision to shut down the unit due to the

uncertainties associated with the core flow data point. Following plant shutdown and

subsequent troubleshooting and investigation, licensee personnel concluded that the

magenta text and suspect note associated with ERIS B33NA01V was an expected system

response. Below approximately 40 percent core flow, the plant process computer shifts the

calculation method from the primary means of calculating core flow using the sum of jet pump

flows to an alternate process that uses core plate differential pressure. As a result of shifting

to the alternate calculation of core flow, data point ERIS B33NA01V was programmed to turn

magenta in color and display suspect to alert operators that the method of calculating core

flow had changed. After this information was disseminated to licensed operators, the

licensee implemented procedural changes to AOP-0024 that provided amplifying information

regarding B33NA01V validated core flow. Specifically, the licensee revised the procedure on

February 7, 2018, in order to provide clear guidance regarding expected system response of

the process computer data points during abnormal flow configurations.

The inspectors compared the actual plant response to the simulator response for the trip of a

recirculation pump while at low power. The actual conditions in the main control room during

the event on February 1, 2018, resulted in ERIS point B33NA01V indicating the correct flow

(27.3Mlbm/hr), but the data point turned magenta in color and displayed the warning label

suspect. This was later determined by information technology personnel to be the correct

response and data display, and was the result of the core flow calculation methodology

swapping from the primary method (jet pump flow) to the alternate method (core plate

differential pressure).

In the simulator, the inspectors determined that ERIS point B33NA01V provided erratic

indications of core flow following a simulated trip of the recirculation pump B from an initial

condition of approximately 25 percent. The indicated flow varied, and ultimately stabilized at

approximately 10Mlbm/hr, which is less than half of the expected indication. Additionally,

B33NA01V did not change to a magenta color, and it did not display the word suspect. The

inspectors determined that ERIS B33NA01V was programmed to calculate core flow using

the sum of jet pump flows at all power levels. As a result, the displayed value was inaccurate

below 40 percent core flow, and the data point was not programmed to turn magenta or

indicate suspect since no swap to a backup means of calculation below 40 percent core

flow was modelled.

22

The inspectors reviewed procedure EN-OP-117, Operations Assessments, Version 4,

Section 5.4, which states that transient snap-shot assessments are performed whenever a

plant transient occurs. A plant transient is defined in section 5.4[2] as including any turbine

generator power change in excess of 10 percent of rated power in less than one minute other

than a momentary spike due to a grid disturbance or a manually initiated runback. The

inspectors concluded that the recirculation pump A trip on December 19, 2012, met the

definition of a transient. EN-OP-117, Attachment 9.2, Transient Snap Shot Assessment

Documentation Form, Objective 7, discusses the training preparation aspect of the

assessment. Specifically, the transient snap-shot assessment is performed in order to

validate that the simulator accurately represented the plant characteristics of the transient.

The licensee provided a Post-Event Simulator Test report that was run on February 14, 2013.

The report concluded that the simulator response matched the parameters observed in the

plant. The inspectors determined that although the snap-shot assessment was performed,

station personnel did not validate that ERIS B33NA01V (validated core flow) provided

operators with the same indications seen by operators in the plant during a recirculation

pump trip.

The inspectors determined that no condition report or simulator deficiency report was

generated to document the discrepancy between the plant and the simulator for displaying

ERIS B33NA01V. The simulator ERIS B33NA01V core flow indication did not display the

correct value for core flow and also did not indicate suspect or turn magenta. The

inspectors reviewed training documentation to determine why this discrepancy was not

observed during continuing simulator training scenarios. The inspectors concluded that this

discrepancy was not documented because the station did not conduct training on abnormal

single loop operations during low power operations. The inspectors reviewed industry

standards and guidelines for simulator training and determined that the station is required to

periodically conduct training on abnormal events that occur during low power operations.

Corrective Actions: The station documented the core flow indication simulator deficiency in a

deficiency report and generated actions to incorporate the discrepancy into future licensed

operator training sessions.

Corrective Action Reference: CR-RBS-2018-03145

Performance Assessment:

Performance Deficiency: The licensees failure to validate core flow in the simulator during a

transient snap shot assessment following the trip of the reactor recirculation pump A on

December 19, 2012, was a performance deficiency.

Screening: The performance deficiency was more than minor, and therefore a finding,

because it was associated with the human performance attribute of the Initiating Events

Cornerstone and adversely affected the cornerstone objective to limit the likelihood of events

that upset plant stability and challenge critical safety functions during shutdown as well as

power operations. Specifically, the failure to validate simulator fidelity following a plant

transient prevented the licensee from identifying simulator model discrepancies when

determining core flow during low power, single loop operations.

23

Significance: The inspectors screened the finding in accordance with Inspection Manual

Chapter 0609, Appendix A, The Significance Determination Process for Findings At-Power.

The finding was determined to be of very low safety significance (Green) because the finding

did not contribute to both the likelihood of a reactor trip and the likelihood that mitigating

equipment would not be available.

Cross-cutting Aspect: No cross cutting aspect was assigned because the performance

deficiency is not indicative of current licensee performance.

Enforcement: Inspectors did not identify a violation of regulatory requirements associated

with this finding.

Failure to Submit a Licensee Event Report for a Manual Scram

Cornerstone

Significance

Cross-cutting

Aspect

Report

Section

None

SLIV

NCV 05000458/2018012-04

Closed

None

71153 -

Follow-up of

Events and

Notices of

Enforcement

Discretion

The inspectors identified a Severity Level IV non-cited violation of 10 CFR 50.73, Licensee

Event Report System, for the licensees failure to submit a required licensee event report

(LER). Specifically, on February 1, 2018, after an unexpected trip of the recirculation pump

B, the licensee initiated a manual scram of the reactor that was not part of a preplanned

sequence and failed to submit an LER within 60 days.

Description: At approximately 9:46 a.m. on February 1, 2018, with the unit operating at

approximately 27 percent power, the recirculation pump B unexpectedly tripped during an

attempted transfer from slow to fast speed. The licensee promptly entered AOP-0024,

Thermal Hydraulic Instability, and GOP-0004, Single Loop Operation. Note 5.8 of AOP-

0024 and Precaution 3.6 of GOP-0004 instruct the licensee to use process computer point

B33NA01V to determine core flow while in single loop operation. The plant process computer

(PPC) and emergency response information system (ERIS) readouts showed conflicting

indications for this computer point, with the PPC showing approximately 13,900 Mlbm/hr of

flow and ERIS showing approximately 26,000 Mlbm/hr of flow.

Step 5.1 of AOP-0024 instructs the licensee to determine where on the power-to-flow map the

plant is operating. If the plant is operating in the restricted region, the procedure states to exit

that region by lowering power or raising flow. If the plant is operating in the exclusion region,

the procedure states to verify that a scram has occurred. The indicated PPC value for core

flow put the plant in an unanalyzed region of the power-to-flow map, with less flow than the

minimum amount of flow that defines any region, including the exclusion region. The

indicated ERIS value put the plant in the restricted region, just above the boundary that

delineates the restricted region from the monitoring region.

The licensee initially believed the ERIS value to be the correct value; however, this value was

accompanied by a magenta suspect note on the ERIS screen, which caused the licensee to

question its validity. In an effort to determine the true value of core flow, the licensee

performed a manual calculation using other known inputs. The licensee performed this

calculation incorrectly and wrongly corroborated the PPC value as the correct value. Given

the inability to establish that the plant was operating in any allowed region of the power-to-

24

flow map, the licensee made the decision to manually actuate the reactor protection system

(RPS) by taking the reactor mode switch to shutdown.

During the investigation after the scram, the licensee determined that the ERIS value was, in

fact, a valid indication of core flow at the time of the event. Operators had not been

adequately trained on the meaning of the magenta suspect indication, and were therefore

unable to determine the implications of the indications on the validity of the data point.

Pursuant to the requirements of 10 CFR 50.72(b)(3)(iv), the licensee reported the scram

event to the NRC at 1:23 p.m. as an event that resulted in an actuation of the RPS. On

March 23, 2018, the licensee retracted the report on the grounds that the actuation was part

of a pre-planned sequence during testing or reactor operation. The inspectors concluded that

this retraction was inappropriate and that the event was reportable for the reasons provided

below.

The inspectors reviewed NUREG-1022, Event Report Guidelines 10 CFR 50.72 and 50.73,

revision 3, which provides the following guidance: Actuations that need not be reported are

those initiated for reasons other than to mitigate the consequences of an event (e.g., at the

discretion of the licensee as part of a preplanned procedure). In the case of the February 1,

2018, River Bend scram event, the inspectors determined that the manual RPS actuation was

initiated in order to mitigate the consequences (i.e., uncertainty as to the condition of the plant

with respect to core flow and power-to-flow considerations) of an event (i.e., the unexpected

loss of a reactor recirculation pump).

NUREG-1022 also provides an example of a reportable manual scram that was event driven

and not part of a preplanned sequence during testing or reactor operation:

At a BWR, both recirculation pumps tripped as a result of a breaker problem. This

placed the plant in a condition in which BWRs are typically scrammed to avoid

potential power/flow oscillations. At this plant, for this condition, a written off-normal

procedure required the plant operations staff to scram the reactor. The plant staff

performed a reactor scram, which was uncomplicated. This event is reportable as a

manual RPS actuation. Even though the reactor scram was in response to an existing

written procedure, this event does not involve a preplanned sequence because the

loss of recirculation pumps and the resultant off-normal procedure entry were event

driven, not preplanned. Both an ENS notification and an LER are required. In this

case, the licensee initially retracted the ENS notification, believing that the event was

not reportable. After staff review and further discussion, it was agreed that the event

is reportable for the reasons discussed above.

As with the scram in the above example, the scram that occurred at River Bend Station was

not part of a preplanned sequence during testing or reactor operation, but was instead an

event driven response to a series of unplanned and unexpected adverse occurrences in the

plant. These occurrences included: a trip of the recirculation pump B, entry into an abnormal

operating procedure for thermal hydraulic instability, an inability to determine core flow and

location on the power-to-flow map in accordance with that procedure, a realization that the

PPC indication of core flow put the plant outside of any allowed operating region of the

power-to-flow map, an incorrect manual calculation that wrongly corroborated the accuracy of

the PPC indication, and the presence of a poorly understood suspect indication that

appeared to undermine the validity of the ERIS flow indication. These adverse occurrences

generated uncertainty as to the status of reactor safety. The subsequent decision to perform

25

a manual reactor scram was consistent with general instruction provided in EN-OP-115,

Conduct of Operations, which states: do not hesitate to reduce power or perform an

immediate reactor shutdown when reactor safety is uncertain. As with the scram in the

above example, the February 1, 2018, River Bend scram also involved entry into an off-

normal procedure due to an unexpected plant equipment malfunction that resulted in the

potential for the plant to be in an undesired condition with respect to power-to-flow

considerations.

The senior resident inspector was present in the control room during the events and was able

to confirm that the shutdown was event driven rather than preplanned. At 10:55 a.m., the

control room briefed that because PPC and ERIS showed conflicting indications of core flow

with ERIS indicating suspect, the mode switch was going to be placed in shutdown. At

10:57 a.m., roughly two minutes after the brief was completed, the reactor operator

scrammed the reactor, and the following station log entry was made: MCR [main control

room] announces placing plant in shut down due to inability to regulate recirculation flow. If

the reactor shutdown had been preplanned, it would not have proceeded at this accelerated

pace. Rather, the licensee would have worked through the relevant steps of the applicable

shutdown procedure, GOP-0004, Single Loop Operation, scramming the reactor only after

those steps had been completed and signed for. Upon review of the copy of GOP-0004 that

was in use by the operators on February 1, 2018, the inspectors noted that no steps of

Attachment 3, Shutdown from Single Loop Operation, were marked as completed, and the

attachment was not signed off as being initiated or completed. The deviation from normal

practice was appropriate because the scram was not being initiated as part of a preplanned

sequence. It was instead being initiated in response to the unanticipated emergence of a

safety concern.

Corrective Actions: The licensee documented the violation in the corrective action program

and generated corrective actions to review reportability requirements.

Corrective Action Reference(s): CR-RBS-2018-03953

Performance Assessment:

Performance Deficiency: The failure to submit a required licensee event report was a

performance deficiency.

Screening: The performance deficiency was evaluated in accordance with the reactor

oversight process and was determined to be minor because it could not be reasonably

viewed as a precursor to a significant event, would not have the potential to lead to a more

significant safety concern, does not relate to a performance indicator that would have caused

the performance indicator to exceed a threshold, and did not adversely affect a cornerstone

objective. The performance deficiency was evaluated in accordance with the traditional

enforcement process because it impacted the ability of the NRC to perform its regulatory

oversight function.

Significance: Using example 6.9.d.9 from the NRC Enforcement Policy, the violation was

determined to be a Severity Level IV violation.

Cross-cutting Aspect: Because the violation was dispositioned using the traditional

enforcement process, no cross-cutting aspect was assigned.

26

Enforcement:

Violation: 10 CFR 50.73(a)(1) requires, in part, that the licensee shall submit a Licensee

Event Report (LER) for any event of the type described in this paragraph within 60 days after

the discovery of the event. 10 CFR 50.73(a)(2)(iv)(A) requires, in part, that the licensee shall

report any event or condition that resulted in manual actuation of the reactor protection

system (RPS) except when the actuation resulted from and was part of a pre-planned

sequence during testing or reactor operation. Contrary to the above, on April 2, 2018, the

licensee failed to submit an LER within 60 days after the discovery of an event or condition

that resulted in manual actuation of the RPS that did not result from and that was not a part of

a pre-planned sequence during testing or reactor operation. Specifically, the licensee failed

to submit an LER within 60 days of a manual reactor scram that occurred on February 1,

2018.

Disposition: Because this SLIV violation was neither repetitive nor willful, and because it was

entered into the licensees corrective action program as Condition Report

CR-RBS-2018-03953, it is being treated as a non-cited violation consistent with

Section 2.3.2.a of the NRC Enforcement Policy.

EXIT MEETINGS AND DEBRIEFS

The inspectors verified no proprietary information was retained or documented in this report.

On May 31, 2018, and on July 16, 2018, the inspectors presented the inspection results to

Mr. W. Maguire, Site Vice President, and other members of the licensee staff.

Attachment

DOCUMENTS REVIEWED

71111.15Operability Determinations and Functionality Assessments

Procedures

Number

Title

Revision

EN-OE-100

Operating Experience Program

12 & 13

STP-051-4206

(RPS Bypassed) RPS/RHR Reactor Vessel Level-Low,

Level 3, High, Level 8, Channel Calibration and Logic

System Functional Test (B21-N680B, B21-N683B, B21-

N080B)

305

STP-051-4227

ECCS/RCIC Actuation Ads Trip System B Reactor

Vessel Water Level Low, Level 3/High, Level 8 Channel

Calibration, and Logic System Functional Test (B21-

N095B, B21-N695B, B21-N693B)

20

STP-501-4202

FWS/MAIN Turbine Trip System - Reactor Vessel Water

Level - High Level 8, Channel Calibration and LSFT

(C33-N004B, C33-K624B, C33-R606B, C33-K650-3)

15

G13.18.6.1.B21

Reactor Vessel Water Level - Low, Level 3 Trip Function

3

G13.18.6.1.B21*003 Reactor Vessel Water Level - Low, Level 3 Trip Function

3

G13.18.6.1.B21*010 Reactor Vessel Water Level - Low, Level 8 Narrow

Range

0, 1, 2, & 3

MCP-IC-501-4202

FWS/FEED Pump Trip System (MSO) - Reactor Vessel

Water Level - High Level 8, Loop Calibration (C33-

LTN006B, C33-ESN606B)

0

71111.18Plant Modifications

Condition Reports (CR-RBS-)

CR-RBS-2014-05194

CR-RBS-2014-06685

CR-RBS-2014-06691

CR-RBS-2015-03253

CR-RBS-2015-03983

CR-RBS-2015-04065

CR-RBS-2015-04117

CR-RBS-2015-08476

CR-RBS-2015-08515

CR-RBS-2016-00791

CR-RBS-2016-00893

CR-RBS-2016-00893

CR-RBS-2016-04351

CR-RBS-2016-04353

CR-RBS-2017-02828

OE-NOE-2004-00008

OE-NOE-2004-00084

Engineering Changes

Number

Title

Revision

EC-75588

Accept As-Is Evaluation for Remainder of Cycle 20: Sparger

N4C Nozzles 7 and 8 Damaged

0 & 1

A-2

Procedures

Number

Title

Revision

OSP-0053

Emergency and Transient Response Support Procedure

20-25

STP-000-0001

Daily Operating Logs

082

DBR-0035279

GEH Comment Resolution Form

0

4221.110-000-

043

Operability Assessment of the River Bend Station

Feedwater Sparger Assembly in the January 2018 As-

Found Condition

0

71152 - Problem Identification and Resolution

Condition Reports (CR-RBS-)

CR-RBS-2018-00358

CR-RBS-2018-00613

CR-RBS-2018-00633

CR-RBS-2018-00733

CR-RBS-2018-00895

CR-RBS-2018-00294

OE-NOE-2004-00008

OE-NOE-2004-00084

Engineering Changes

Number

Title

Revision

EC-75663

Loose Parts Evaluation for Material Lost From

Feedwater Spargers Identified During PO-18-01

Foreign Material FME LPA-000

0

Miscellaneous Documents

Number

Title

Revision/Date

OSRC Meeting 2018-0001 Minutes

OSRC Meeting 2018-0002 Minutes

Action Item OE33308-20110507-A2-RBS-001

CNR RBS PO-18-01-01 Foreign Material Customer Notification Report

0

ECH-NE-17-00039

River Bend MOC-20a Fuel Inspection Plan

0

NEDC-31336P-A

General Electric Instrument Setpoint

Methodology

0

NEDE-21821-A

Boiling Water Reactor Feedwater

Nozzle/Sparger Final Report

0

NEI 96-07

Guidelines for 10 CFR 50.59 Implementation

1

OE33308-20110507

Sampling Probe Found in Feedwater Sparger

August 17, 2011

A-3

Miscellaneous Documents

Number

Title

Revision/Date

PO 18-01

BOP Foreign Material Inspection Report

RBS-ER-99-0539

Engineering Response Associated with Loose

Part in the Feedwater System

0

Procedures

Number

Title

Revision

AOP-0001

Reactor Scram

37

AOP-0024

Thermal Hydraulic Stability Controls

30, 31, & 32

EN-NF-102

Corporate Fuel Reliability

6

EN-OP-104

Operability Determination Process

14

EN-OP-111

Operational Decision Making Issue Process

15

EN-OP-117

Operations Assessments

4

EOP-0001

Emergency Operating Procedure - RPV Control

28

GOP-0001

Plant Startup

99

GOP-0002

Power Decrease/Plant Shutdown

78

GOP-0003

Scram Recovery

31

GOP-0004

Single Loop Operation

25

OE-100

Operating Experience Program

1

R-PL-012

Corrective Action Program

1

STP-000-0001

Daily Operating Logs

082

Work Order 52599498

71153Follow-up of Events and Notices of Enforcement Discretion

Procedures

Number

Title

Revision

EN-OP-115

Conduct of Operations

23

GOP-0004

Single Loop Operation

23

Condition Reports (CR-RBS-)

2018-03149

2018-03953

ML18194A413

SUNSI Review:

ADAMS:

Non-Publicly Available

Non-Sensitive

Keyword:

By: CHY/RDR

Yes No

Publicly Available

Sensitive

NRC-002

OFFICE

SRI:DRP/C

RI:DRP/C

SPE:DRP/C

ARI:DRP/C

C:DRS/EB2

D:DRP

NAME

JSowa

BParks

CYoung

MOBanion

JDrake

AVegel

SIGNATURE

/RA/

/RA/

/RA/

/RA/

/RA/

/RA/

DATE

6/22/2018

6/21/2018

6/21/2018

6/25/2018

7/10/2018

7/18/18

OFFICE

BC:DRP/C

NAME

JKozal

SIGNATURE

/RA/

DATE

7/18/18