ML19320B080: Difference between revisions

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Jersey Central Power ta Light Company
[y Jersey Central Power ta Light Company
[y  4-(') f                                                 Madison Avenue at Punch Bowl Road Momstown, New Jersey 07960 (201)455-8200 July 2, 1980 Director Nuclear Reactor Regulation JJ. S. Nuclear Regulatory Commission Washington, D. C.                 20555
(') f 4-Madison Avenue at Punch Bowl Road Momstown, New Jersey 07960 (201)455-8200 July 2, 1980 Director Nuclear Reactor Regulation JJ. S. Nuclear Regulatory Commission Washington, D. C.
20555


==Dear Sir:==
==Dear Sir:==
==Subject:==
==Subject:==
Oyster Creek Nuclear Generating Station Docket No. 50-219 Fire Protection - Alternate Water Supply In accordance                   Oyster Creek Nuclear Generating Station Operating License No. 7                     , paragraph 3.E, the purpose of this correspondence is to notify you of a slippage in the implementation schedule for the installation of the Alternate Water Supply indicated in Table 3.1 item 3.1.20 of the NRC Safety Evaluation Report (SER).
Oyster Creek Nuclear Generating Station Docket No. 50-219 Fire Protection - Alternate Water Supply In accordance Oyster Creek Nuclear Generating Station Operating License No. 7
The slippage has been caused by engineering problems associated with the installation, and manpower probleas due to the current refueling outage and *INI lessons learned work. The installation of the new water supply requires cleaning an existing tank which has not been available due to the unforeseen extension of the current refueling outage. Additionally, due to the exterded outage and the work associated with TMI lessons learned,                                               !
, paragraph 3.E, the purpose of this correspondence is to notify you of a slippage in the implementation schedule for the installation of the Alternate Water Supply indicated in Table 3.1 item 3.1.20 of the NRC Safety Evaluation Report (SER).
personnel resources ~have been limited. This situa' tion was discussed                                                    i during a meeting between Mr. J. Knubel, Supervisor-Nuclear Safety 6                                                       i Licensing, and your staff on May 28, 1980.                                                                                 I 1
The slippage has been caused by engineering problems associated with the installation, and manpower probleas due to the current refueling outage and *INI lessons learned work. The installation of the new water supply requires cleaning an existing tank which has not been available due to the unforeseen extension of the current refueling outage. Additionally, due to the exterded outage and the work associated with TMI lessons learned, This situa' ion was discussed personnel resources ~have been limited.
t during a meeting between Mr. J. Knubel, Supervisor-Nuclear Safety 6 Licensing, and your staff on May 28, 1980.
In conclusion, the Alternate Water Supply to the yard loop will be completed prior to November 1, 1980, which is in accordance with the currently proposed revisions to 10CFR50 (addition of new Section 50.48 and a new Appendix R).
In conclusion, the Alternate Water Supply to the yard loop will be completed prior to November 1, 1980, which is in accordance with the currently proposed revisions to 10CFR50 (addition of new Section 50.48 and a new Appendix R).
Very truly yours, th{ . AW Ivan R. Fi         oc , Jr.
Very truly yours, th{. AW Ivan R. Fi oc, Jr.
Vice President
Vice President
          - la 8007090$ @                     I Jersey Central Power & Ught Company is a Member of the General Pubhc Ut Aties System}}
- la 8007090$ @ I Jersey Central Power & Ught Company is a Member of the General Pubhc Ut Aties System}}

Latest revision as of 18:42, 1 January 2025

Notifies of Delay in Implementation Schedule for Installation of Alternate Water Supply Per Safety Evaluation Table 3.1.Caused by Engineering & Manpower Problems.Alternate Water Supply Will Be Completed by 801101
ML19320B080
Person / Time
Site: Oyster Creek
Issue date: 07/02/1980
From: Finfrock I
JERSEY CENTRAL POWER & LIGHT CO.
To:
Office of Nuclear Reactor Regulation
References
NUDOCS 8007090262
Download: ML19320B080 (6)


Text

._

[y Jersey Central Power ta Light Company

(') f 4-Madison Avenue at Punch Bowl Road Momstown, New Jersey 07960 (201)455-8200 July 2, 1980 Director Nuclear Reactor Regulation JJ. S. Nuclear Regulatory Commission Washington, D. C.

20555

Dear Sir:

Subject:

Oyster Creek Nuclear Generating Station Docket No. 50-219 Fire Protection - Alternate Water Supply In accordance Oyster Creek Nuclear Generating Station Operating License No. 7

, paragraph 3.E, the purpose of this correspondence is to notify you of a slippage in the implementation schedule for the installation of the Alternate Water Supply indicated in Table 3.1 item 3.1.20 of the NRC Safety Evaluation Report (SER).

The slippage has been caused by engineering problems associated with the installation, and manpower probleas due to the current refueling outage and *INI lessons learned work. The installation of the new water supply requires cleaning an existing tank which has not been available due to the unforeseen extension of the current refueling outage. Additionally, due to the exterded outage and the work associated with TMI lessons learned, This situa' ion was discussed personnel resources ~have been limited.

t during a meeting between Mr. J. Knubel, Supervisor-Nuclear Safety 6 Licensing, and your staff on May 28, 1980.

In conclusion, the Alternate Water Supply to the yard loop will be completed prior to November 1, 1980, which is in accordance with the currently proposed revisions to 10CFR50 (addition of new Section 50.48 and a new Appendix R).

Very truly yours, th{. AW Ivan R. Fi oc, Jr.

Vice President

- la 8007090$ @ I Jersey Central Power & Ught Company is a Member of the General Pubhc Ut Aties System