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Duke Power Company (704)875-4000 McGuire Nudear Station 12700 Hagers Ferry Road Hunterstalle, NC 28078 R935 DUKE POWER November 22, 1994 U.S. Nuclear Regulatory Commission Document Control Desk Washington, D.C. | |||
20555 | |||
==Subject:== | ==Subject:== | ||
McGuire Nuclear Station Unit 1 Special Report No. 94-05 Problem Investigation Process No.: 1-M94-1620 Gentlemen: | McGuire Nuclear Station Unit 1 Special Report No. 94-05 Problem Investigation Process No.: 1-M94-1620 Gentlemen: | ||
Attached is a Special Report concerning Channel 3 of the Vibration and Loose Parts Monitoring System being found inoperable. This report is being submitted per Technical Specification 3.3.10 and 6.9.2. This event is considered to be of no significance with respect to the health and safety of the public. | Attached is a Special Report concerning Channel 3 of the Vibration and Loose Parts Monitoring System being found inoperable. | ||
This report is being submitted per Technical Specification 3.3.10 and 6.9.2. | |||
This event is considered to be of no significance with respect to the health and safety of the public. | |||
-Very truly yours, Y' | |||
.C. McMeekin RJD/bcb Attachment xc: | |||
Mr. | |||
S.D. | |||
Ebneter INPO Records Center Administrator, Region II Suite 1500 U.S. Nuclear Regulatory Commission 1100 Circle 75 Parkway 101 21arietta St., | |||
nes er ~:yw s,w | NW, Suite 2900 Atlanta, GA 30339 Atlanta, GA 30323 Mr. Victor Nerses Mr. George Maxwell U.S. Nuclear Regulatory Commission NRC Resident Inspector Office of Nuclear Reactor Regulation McGuire Nuclear Station Washington, D.C. | ||
20555 94113co34g 94y12, R | |||
S ADOCK 05000$69 | |||
.} I PDR v | |||
4 O U U.b $ | |||
\\ | |||
nes er ~:yw s,w | |||
c 4 | |||
bxc: B.L. Walsh'(EC11C) | bxc: | ||
B.L. Walsh'(EC11C) | |||
P.R. Herran (MG01VP) | |||
I R.* C. Norcutt (MG01WC) i K.L. Crane (MG01RC) | |||
B.F. Caldwell (MG01VP) | |||
R.N. Casler (EC05N) | R.N. Casler (EC05N) | ||
S.G. Benesole (ONO3RC) | S.G. | ||
G.H. Savage (EC06E) | Benesole (ONO3RC) | ||
G.H. | |||
Savage (EC06E) | |||
G.B. Swindlehurst (EC11-0842) | G.B. Swindlehurst (EC11-0842) | ||
M.S. Tuckman (EC07H) | M.S. Tuckman (EC07H) | ||
| Line 50: | Line 64: | ||
S r | S r | ||
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j Special Report SR-94-05 Unit i Vibration and Loose Parts Monitor Operability of Channel 3 Associated Technical Specification: | j Special Report SR-94-05 Unit i Vibration and Loose Parts Monitor Operability of Channel 3 Associated Technical Specification: | ||
October 24,1994 at 0500 Hrs. (TSAIL entry Ml-094-01135) due to noise. WR 94043758 was written to troubleshoot the problem. IAE investigated and identified the pmblem, however, the system is located in a high radiation area and this channel is not required for plant operation. | 3.3.3.10 Related PIP: | ||
Instmment Vendor: | 1-M94-1620 Cause of Malfunction: | ||
Generic Concems: | Channel 3 (EMD ME 9000) of the Unit i Vibration and Loose Parts Monitor was declared INOPERABLE by Operations on October 24,1994 at 0500 Hrs. (TSAIL entry Ml-094-01135) due to noise. WR 94043758 was written to troubleshoot the problem. IAE investigated and identified the pmblem, however, the system is located in a high radiation area and this channel is not required for plant operation. | ||
of NSM MG-12096, replacement of the entim system, which will be completed during. | Instmment Vendor: | ||
V& LPM manufactured by Rockwell Intemational. | |||
Generic Concems: | |||
The V& LPM has a history of unreliable performance. Numerous sensor and cable problems are the main contributor to this unreliable performance. These concems are being addressed by the panial completion of NSM MG-12096, replacement of the entim system, which will be completed during. | |||
1EOC10. Installation during iEOC9 was delayed because of vendor equipment delivery. | 1EOC10. Installation during iEOC9 was delayed because of vendor equipment delivery. | ||
Compensatory Measures: | Compensatory Measures: | ||
Operability Restoration: | No compensatory measures are planned or required. | ||
Future Plans: | Operability Restoration: | ||
Channel 3 of the V& LPM will be repaired under WR 94043758 or replaced by NSM MG-12096 during outage IEOC10. | |||
Date: /[' E ~ | Future Plans: | ||
Both Unit I and Unit 2 V&LPMs will be replaced by new and enhanced analysis equipment. The senson; and cables will be replaced at the same time. | |||
/k Date: //- 22-M By: | |||
m Approval: M Date: /[' E ~ | |||
~ | |||
- _.}} | |||
Latest revision as of 00:25, 15 December 2024
| ML20078L657 | |
| Person / Time | |
|---|---|
| Site: | McGuire |
| Issue date: | 11/22/1994 |
| From: | Mcmeekin T DUKE POWER CO. |
| To: | NRC OFFICE OF INFORMATION RESOURCES MANAGEMENT (IRM) |
| References | |
| SR-94-05, SR-94-5, NUDOCS 9411300348 | |
| Download: ML20078L657 (3) | |
Text
.. _.
ll l
Duke Power Company (704)875-4000 McGuire Nudear Station 12700 Hagers Ferry Road Hunterstalle, NC 28078 R935 DUKE POWER November 22, 1994 U.S. Nuclear Regulatory Commission Document Control Desk Washington, D.C.
20555
Subject:
McGuire Nuclear Station Unit 1 Special Report No. 94-05 Problem Investigation Process No.: 1-M94-1620 Gentlemen:
Attached is a Special Report concerning Channel 3 of the Vibration and Loose Parts Monitoring System being found inoperable.
This report is being submitted per Technical Specification 3.3.10 and 6.9.2.
This event is considered to be of no significance with respect to the health and safety of the public.
-Very truly yours, Y'
.C. McMeekin RJD/bcb Attachment xc:
Mr.
S.D.
Ebneter INPO Records Center Administrator, Region II Suite 1500 U.S. Nuclear Regulatory Commission 1100 Circle 75 Parkway 101 21arietta St.,
NW, Suite 2900 Atlanta, GA 30339 Atlanta, GA 30323 Mr. Victor Nerses Mr. George Maxwell U.S. Nuclear Regulatory Commission NRC Resident Inspector Office of Nuclear Reactor Regulation McGuire Nuclear Station Washington, D.C.
20555 94113co34g 94y12, R
S ADOCK 05000$69
.} I PDR v
4 O U U.b $
\\
nes er ~:yw s,w
c 4
bxc:
B.L. Walsh'(EC11C)
P.R. Herran (MG01VP)
I R.* C. Norcutt (MG01WC) i K.L. Crane (MG01RC)
B.F. Caldwell (MG01VP)
R.N. Casler (EC05N)
S.G.
Benesole (ONO3RC)
G.H.
Savage (EC06E)
G.B. Swindlehurst (EC11-0842)
M.S. Tuckman (EC07H)
R.F. Cole (EC05N).
D.B. Cook (EC13A)
G.A. Copp (EC050)
Tim Becker (PB02L)
J.I. Glenn (MG02ME)
P.M. Abraham (EC081)
Zach Taylor (CN01RC)
L.V. Wilkie (ON05SR)
D.P. Kimball (CNO3SR)
NSRB Support Staff (EC05N)
S r
d
.r.
j Special Report SR-94-05 Unit i Vibration and Loose Parts Monitor Operability of Channel 3 Associated Technical Specification:
3.3.3.10 Related PIP:
1-M94-1620 Cause of Malfunction:
Channel 3 (EMD ME 9000) of the Unit i Vibration and Loose Parts Monitor was declared INOPERABLE by Operations on October 24,1994 at 0500 Hrs. (TSAIL entry Ml-094-01135) due to noise. WR 94043758 was written to troubleshoot the problem. IAE investigated and identified the pmblem, however, the system is located in a high radiation area and this channel is not required for plant operation.
Instmment Vendor:
V& LPM manufactured by Rockwell Intemational.
Generic Concems:
The V& LPM has a history of unreliable performance. Numerous sensor and cable problems are the main contributor to this unreliable performance. These concems are being addressed by the panial completion of NSM MG-12096, replacement of the entim system, which will be completed during.
1EOC10. Installation during iEOC9 was delayed because of vendor equipment delivery.
Compensatory Measures:
No compensatory measures are planned or required.
Operability Restoration:
Channel 3 of the V& LPM will be repaired under WR 94043758 or replaced by NSM MG-12096 during outage IEOC10.
Future Plans:
Both Unit I and Unit 2 V&LPMs will be replaced by new and enhanced analysis equipment. The senson; and cables will be replaced at the same time.
/k Date: //- 22-M By:
m Approval: M Date: /[' E ~
~
- _.