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                                                                                          '
O.S. NUCLEAR REGULATORY COMMISSION
    .
!
                              O.S. NUCLEAR REGULATORY COMMISSION
'
                                                                                            !
REGION II
                                                                                          '
1
                                              REGION II
Docket Nos:
                                                                                          1
50-321, 50-366
                  Docket Nos:         50-321, 50-366                                     I
License Nos:
                  License Nos:         DPR-57 and NPF-5                                   !
DPR-57 and NPF-5
                                                                                          :
!
                                                                                          :
:
                  Report No:           50-321/96-15, 50-366/96-15                         l
:
                                                                                          !
Report No:
                                                                                          1
50-321/96-15, 50-366/96-15
                                                                                          !
l
                  Licensee:           Georgia Power Company (GPC)
!
                                                                                          i
1
                                                                                          i
Licensee:
                  Facility:           E. I. Hatch Units 1 & 2                           l
Georgia Power Company (GPC)
                                                                                          !
i
                  Location:           P. O. Box 439                                     i
i
                                        Baxley' Georgia 31513                             :
Facility:
                  Dates:               December 8, 1996 - January 18, 1997
E. I. Hatch Units 1 & 2
                  Inspectors:   B. Holbrook. Senior Resident Inspector
!
                                  E. Christnot. Resident Inspector
Location:
                                  J. Canady. Resident Inspector
P. O. Box 439
                                  G. Kuzo. Senior Radiation Specialist (Sections
i
                                        R1.2 - R8.2)~.
Baxley' Georgia 31513
                                  W. Kleinsorge Reactor Inspector (Section M1.4)
:
                  Approved by:   P. Skinner. Chief. Projects Branch 2
Dates:
                                        Division of Reactor Projects
December 8, 1996 - January 18, 1997
                                                                            Enclosure 2
Inspectors:
      9702190262 970213
B. Holbrook. Senior Resident Inspector
      PDR ADOCK 05000321
E. Christnot. Resident Inspector
    0               PDR
J. Canady. Resident Inspector
G. Kuzo. Senior Radiation Specialist (Sections
R1.2 - R8.2)~.
W. Kleinsorge Reactor Inspector (Section M1.4)
Approved by:
P. Skinner. Chief. Projects Branch 2
Division of Reactor Projects
Enclosure 2
9702190262 970213
PDR
ADOCK 05000321
0
PDR


  0
0
    *
*
,
,
                                  EXECUTIVE SUMMARY
EXECUTIVE SUMMARY
                              Plant Hatch Units 1 and 2
Plant Hatch Units 1 and 2
                  NRC Inspection Report 50-321/96-15, 50-366/96-15
NRC Inspection Report 50-321/96-15, 50-366/96-15
      This integrated inspection included aspects of licensee operations,
This integrated inspection included aspects of licensee operations,
      engineering, maintenance, and plant support. The report covers a 6-week
engineering, maintenance, and plant support. The report covers a 6-week
      period of resident inspection. In addition, it includes the results of
period of resident inspection.
      an announced inspection by a regional Senior Radiation Specialist and a
In addition, it includes the results of
      Reactor Engineer's inspection of electrical maintenance.
an announced inspection by a regional Senior Radiation Specialist and a
      Ooerations
Reactor Engineer's inspection of electrical maintenance.
      e      The inspectors concluded that Unit 2 control room operator's
Ooerations
            demonstrated a lack of attention to detail during control room
The inspectors concluded that Unit 2 control room operator's
            panel walkdowns. Operators did not observe an incorrect switch
e
            position and a keepfill pump that had automatically started
demonstrated a lack of attention to detail during control room
            (Section 01.2).
panel walkdowns.
      e     The inspectors identified as a strength operations management's
Operators did not observe an incorrect switch
            proactive actions with respect to providing operator training to
position and a keepfill pump that had automatically started
            correct or prevent some deficiencies (Secticn 05.1).
(Section 01.2).
      e     The inspectors concluded that the shift of operators reviewed for
e
            fire fighting and fire brigade leader training and qualifications
The inspectors identified as a strength operations management's
            were trained and qualified for their assigned position.
proactive actions with respect to providing operator training to
            Corrective lenses for o)erator use while wearing Self Contained
correct or prevent some deficiencies (Secticn 05.1).
            Breathing Apparatus (SC3A) during control room emergencies were
e
            readily available in the control room (Sectiori 05.2).
The inspectors concluded that the shift of operators reviewed for
      e     The inspectors concluded that plant procedures did not include
fire fighting and fire brigade leader training and qualifications
            guidance for removing valves from backseat following plant
were trained and qualified for their assigned position.
            transient conditions that resulted in a reactor cooldown. This
Corrective lenses for o)erator use while wearing Self Contained
            was identified as a weakness. After inspector intervention, the
Breathing Apparatus (SC3A) during control room emergencies were
            additional guidance and expectations provided to operators during
readily available in the control room (Sectiori 05.2).
            shift briefings were appropriate (Section M3.2).
e
      e     The inspectors concluded that the operations department
The inspectors concluded that plant procedures did not include
            demonstrated a commitment to self assessment and a desire for
guidance for removing valves from backseat following plant
            continued improvement. Although some corrective recunmendations
transient conditions that resulted in a reactor cooldown.
            contained in the self assessment were not completed, they were
This
            under development and the completed items were thorough and
was identified as a weakness.
            comprehensive. The self assessments were conducted by
After inspector intervention, the
            knowledgeable personnel (Section 07.1).
additional guidance and expectations provided to operators during
                                                                      Enclosure 2
shift briefings were appropriate (Section M3.2).
e
The inspectors concluded that the operations department
demonstrated a commitment to self assessment and a desire for
continued improvement.
Although some corrective recunmendations
contained in the self assessment were not completed, they were
under development and the completed items were thorough and
comprehensive.
The self assessments were conducted by
knowledgeable personnel (Section 07.1).
Enclosure 2


  ., .y _             _                             _ _       _._       _       _
.,
                                                                                        . _ _ . ,
.y
                                                                                                  I
_
      "
_
.,                                                                                               J
_ _
                                                                                                  l
_._
                                              2                                                  :
_
          e     The failure of the traveling water screen system to operate during
_
                cold weather conditions is identified as a significant weakness in
. _ _ . ,
                the area of engineering. Engineering personnel failed to identify
J
                that the design and system configuration did not adequately ~
"
                  3rotect system components from cold weather conditions.                         <
.,
                  iaintenance and operations personnel also failed to identify that               '
2
                portions of the system were vulnerable to cold weather conditions
:
                during their system checks and cold weather preparations                         !
e
                  (Section 08.1),                                                                 j
The failure of the traveling water screen system to operate during
          Maintenance                                                                           j
cold weather conditions is identified as a significant weakness in
                                                                                                  !
the area of engineering.
          e     The ins)ectors concluded that the maintenance work activities and               i
Engineering personnel failed to identify
                the worc review by the system engineer for the IB Emergency Diesel               i
that the design and system configuration did not adequately ~
                                                                                                  '
3rotect system components from cold weather conditions.
                Generator (EDG) voltage regulator re) air were thorough and
<
                performed in accordance with applica)1e procedures. Supervisory                 ;
'
                and engineering oversight were evident. The inspectors also                     i
iaintenance and operations personnel also failed to identify that
                concluded that the EDG design function capability was not degraded               -
portions of the system were vulnerable to cold weather conditions
                  (Section M1.2).                                                                 >
during their system checks and cold weather preparations
                                                                                                  :
!
          e     The ins)ectors concluded that the maintenance activities on the                 '
(Section 08.1),
                Unit 2 Reactor Core Isolation Cooling turbine identified and                     ;
j
                corrected the problem with the fluctuations in turbine speed                     l
Maintenance
                control. Maintenance activities observed were generally thorough                 i
j
                and professional. Supervisory and engineering oversight were                     ;
!
                evident (Section M1.3).                                                         J
e
                                                                                                  t
The ins)ectors concluded that the maintenance work activities and
          e     The inspectors identified an Inspector Followup Item (IFI)
i
                50-321, 366/96-15-04:   Switchyard Maintenance and Material
the worc review by the system engineer for the IB Emergency Diesel
                Condition. This was due to the switchyard housekeeping and
i
                material condition discrepancies and the number and age of the
'
                predictive maintenance backlogged items for the switchyard
Generator (EDG) voltage regulator re) air were thorough and
                (Section M1.4).
performed in accordance with applica)1e procedures.
          e     As demonstrated by good performance, the level of 3reventive
Supervisory
                maintenance for the Reactor Protection System and Reactor
;
                Recirculation System Motor Generator Sets was appropriate for the
and engineering oversight were evident.
                circumstances (Section M1.4).
The inspectors also
          e     The lack of records that support differences from equipment
i
                manufacturers' 3reventive maintenance recommendations and
concluded that the EDG design function capability was not degraded
                dependance on t1e collective memory of personnel was not a good
-
                practice (Section M1.4).
(Section M1.2).
          e     Leaving loose conductive material in electrical panels was
>
                identified as a poor work practice for foreign material exclusion
:
                control with the potential of shorting out components. Some                       j
'
                housekeeping discrepancies were noted (Section M1.4).                             i
e
                                                                            Enclosure 2
The ins)ectors concluded that the maintenance activities on the
Unit 2 Reactor Core Isolation Cooling turbine identified and
;
corrected the problem with the fluctuations in turbine speed
l
control.
Maintenance activities observed were generally thorough
i
and professional.
Supervisory and engineering oversight were
;
evident (Section M1.3).
J
t
e
The inspectors identified an Inspector Followup Item (IFI)
50-321, 366/96-15-04:
Switchyard Maintenance and Material
Condition. This was due to the switchyard housekeeping and
material condition discrepancies and the number and age of the
predictive maintenance backlogged items for the switchyard
(Section M1.4).
e
As demonstrated by good performance, the level of 3reventive
maintenance for the Reactor Protection System and Reactor
Recirculation System Motor Generator Sets was appropriate for the
circumstances (Section M1.4).
e
The lack of records that support differences from equipment
manufacturers'
3reventive maintenance recommendations and
dependance on t1e collective memory of personnel was not a good
practice (Section M1.4).
e
Leaving loose conductive material in electrical panels was
identified as a poor work practice for foreign material exclusion
control with the potential of shorting out components.
Some
j
housekeeping discrepancies were noted (Section M1.4).
i
Enclosure 2


--.   . - - -- .
--.
    '
. - - --
.
'
.
.
                                                3
3
                e The inspectors identified Non-Cited Violation (NCV)
e
                    50-366/96-15-01: Inadequate Procedures for Replacement of the
The inspectors identified Non-Cited Violation (NCV)
                    Unit 2 Drywell Hydrogen Recombiner Flow Controller Batteries and
50-366/96-15-01:
                    Establishing the Required Controller " Dead Band" Following Certain
Inadequate Procedures for Replacement of the
                  Maintenance Activities (Section M2.1).
Unit 2 Drywell Hydrogen Recombiner Flow Controller Batteries and
                e Operator performance during surveillance activities for the High
Establishing the Required Controller " Dead Band" Following Certain
                    Pressure Coolant Injection System and EDG was generally
Maintenance Activities (Section M2.1).
                  professional and competent. The inspectors had observed some
e
                    improvements in communications in the recent past but observed
Operator performance during surveillance activities for the High
                  that operations * standards were not met by all crews
Pressure Coolant Injection System and EDG was generally
                    (Section M3.1)
professional and competent. The inspectors had observed some
                e The inspectors identified Violation (VIO) 50-321/96-15-02:
improvements in communications in the recent past but observed
                  Maintenance Personnel Failure To Follow Procedure During Valve
that operations * standards were not met by all crews
                  Backseating Activities. This failure to follow procedure was
(Section M3.1)
                  generally administrative in nature (Section M3.2).
e
                * The inspectors also concluded that some maintenance personnel's
The inspectors identified Violation (VIO) 50-321/96-15-02:
                    lack of understanding of different types of procedure usage and
Maintenance Personnel Failure To Follow Procedure During Valve
                    implementation demonstrated a weakness (Section M3.2).
Backseating Activities. This failure to follow procedure was
                e The inspectors concluded that the maintenance procedure for
generally administrative in nature (Section M3.2).
                  electrically backseating valves did not fully implement the
*
                  requirements of the engineering evaluation. The inspectors
The inspectors also concluded that some maintenance personnel's
                  concluded that this deficiency did not result in a
lack of understanding of different types of procedure usage and
                  safety-significant concern for the backseated valves
implementation demonstrated a weakness (Section M3.2).
                    (Section M3.2).
e
                e Inspector Followup Item (IFI) 50-321. 366/96-15-03: Resolution of
The inspectors concluded that the maintenance procedure for
                  Reactor Core Isolation Cooling (RCIC) and High Pressure Coolant
electrically backseating valves did not fully implement the
                  Injection System (HPCI) Turbine Speed Control Drifting, for
requirements of the engineering evaluation. The inspectors
                  Units 1 and 2. respectively, was identified. The inspectors
concluded that this deficiency did not result in a
                  concluded that the maximum speed drift observed on the both
safety-significant concern for the backseated valves
                  systems did not affect the safety function of either system. The
(Section M3.2).
                  inspectors concluded that the speed control drifting could be an
e
                  indication of pending failures (Section M3.3).
Inspector Followup Item (IFI) 50-321. 366/96-15-03:
                e The inspectors concluded that the Unit 2 loss of feedwater heating
Resolution of
                  transient on January 5. due to a jumper grounding error,
Reactor Core Isolation Cooling (RCIC) and High Pressure Coolant
                  demonstrated a poor work practice on the part of one individual.
Injection System (HPCI) Turbine Speed Control Drifting, for
                  This problem was identified as an isolated occurrence and not a
Units 1 and 2. respectively, was identified. The inspectors
                  generic concern. Reviewing this error for human performance
concluded that the maximum speed drift observed on the both
                  improvements was appropriate (Section M4.1).
systems did not affect the safety function of either system.
                * Personnel who perform mechanical maintenance on safety and non-
The
                  safety related valves were trained and qualified in accordance
inspectors concluded that the speed control drifting could be an
                  with the requirements of ANSI N18.1-1971, the Final Safety
indication of pending failures (Section M3.3).
                  Analysis Report, and other applicable plant qualification
e
                  procedures (Section M5.1).
The inspectors concluded that the Unit 2 loss of feedwater heating
                                                                            Enclosure 2
transient on January 5. due to a jumper grounding error,
                                                                                        ____J
demonstrated a poor work practice on the part of one individual.
This problem was identified as an isolated occurrence and not a
generic concern. Reviewing this error for human performance
improvements was appropriate (Section M4.1).
*
Personnel who perform mechanical maintenance on safety and non-
safety related valves were trained and qualified in accordance
with the requirements of ANSI N18.1-1971, the Final Safety
Analysis Report, and other applicable plant qualification
procedures (Section M5.1).
Enclosure 2
J


          . ~ . . ~ - s . . .             s.,_.. a -~.w - ---.   .w - - .n   n . . , - - . . .--..n.- -a ..~. .- a. . _ -. - ~ .
=.-3
    =.-3                          .
. ~ . . ~ -
                                    - . -                                    ..
s
. . .
.
. -
s.,_..
a
-~.w
- ---.
.w
- -
.n
..
n
. . , - - . .
.--..n.-
-a
..~. .-
a. . _ -. - ~ .
-
.
.
  ,      .
.
      ,
,
,                                                                 4
,
                      Enaineerina                                                                                                    i
4
4
                                                                                                                                      :
,
;                      e        The inspectors concluded that the Unit 1 Standby Liquid Control                                      i
Enaineerina
                                                                                                                                      '
i
:
:
                                (SLC) pump tripping was an isolated problem. The inspectors
4
                                concluded that engineering personnel from the Nuclear Safety And                                     3
The inspectors concluded that the Unit 1 Standby Liquid Control
i
;
e
'
(SLC) pump tripping was an isolated problem. The inspectors
:
concluded that engineering personnel from the Nuclear Safety And
3
l
l
Compliance (NS&C) conducted a detailed review of the SLC pump
tripping problem, and was viewed as a positive attribute of the
'
'
                                Compliance (NS&C) conducted a detailed review of the SLC pump
j
                                tripping problem, and was viewed as a positive attribute of the
department. Replacement of the system components was appropriate
j                              department. Replacement of the system components was appropriate
(Section E2.1).
                                (Section E2.1).
4
4                                                                                                                                     :
:
                      e        The inspectors concluded that the engineering evaluation for                                         !
The inspectors concluded that the engineering evaluation for
!
e
electrically backseating valves located in the drywell was
.
,
satisfactory. The evaluation considered plant safety and
!
.
identified actions to ensure continued system and component
:
>
reliability (Section E3.1).
Plant Suooort
,
,
                                electrically backseating valves located in the drywell was                                            .
The inspectors identified a Violation 50-321, 366/96-15-05:
.                              satisfactory. The evaluation considered plant safety and                                             !
:
>                              identified actions to ensure continued system and component                                          :
J
                                reliability (Section E3.1).
e
2
Failure to Follow Procedures for Contamination Control and for
;
!
Deficiency Card Issuance for Inadequate Bioassay Calibration
i
i
Guidance. Quality control cross-check analyses were conducted in
;
accordance with procedural requirements (Sections R1.2 and R7.1).
!
,
,
                      Plant Suooort
J                      e        The inspectors identified a Violation 50-321, 366/96-15-05:                                          :
2                              Failure to Follow Procedures for Contamination Control and for                                        ;
!                              Deficiency Card Issuance for Inadequate Bioassay Calibration                                          i
i                              Guidance. Quality control cross-check analyses were conducted in                                      ;
,                              accordance with procedural requirements (Sections R1.2 and R7.1).                                    !
.
.
                                                                                                                                      ,
,
j                     e       General employee training and completed medical certifications for                                   i
j
2                              personnel involved in licensed activities were conducted in                                           <
e
!                               accordance with the anlicable procedures and met the requirements
General employee training and completed medical certifications for
L                               of 10 CFR 19 and 10 C 120 (Section R.5).
i
personnel involved in licensed activities were conducted in
2
<
!
accordance with the anlicable procedures and met the requirements
L
of 10 CFR 19 and 10 C 120 (Section R.5).
4
4
;                     e       Radiation protection performance indicators verified that licensee
;
,                              actions to control worker dose were effective and radiological                                       ,
e
Radiation protection performance indicators verified that licensee
actions to control worker dose were effective and radiological
,
,
effluent releases were minimized (Section R8).
i
,
,
                                effluent releases were minimized (Section R8).                                                        i
.
.
3
3
                      o       The inspectors concluded that the inspected areas of the security                                     ,
o
                                                                                                                                      '
The inspectors concluded that the inspected areas of the security
                                program met the applicable requirements (Section S2).
,
)                     e        The inspectors attended various Outage Management Meetings held at
'
  ;                             the site and concluded that the critical path for the refueling                                       ;
program met the applicable requirements (Section S2).
j                               outage was identified and that the refueling outage appeared to be                                   ;
)
                                well planned, with realistic goals and adequate support
The inspectors attended various Outage Management Meetings held at
e
;
the site and concluded that the critical path for the refueling
;
j
outage was identified and that the refueling outage appeared to be
;
well planned, with realistic goals and adequate support
.
.
                                (Section X.2).                                                                                       ,
(Section X.2).
,
-
-
i
i
                                                                                                                                      ;
;
  ;
;
;                                                                                                   Enclosure 2                       ,
;
                                                                                                                                      I
Enclosure 2
  :
,
.
:
                                                                                                                                -
.
. -
-
-
-
. .. . - -
-
.-..
-


  .
    *
.
.
                                  Reoort Details
*
      Summary of Plant Status
.
      Unit 1 operated at 100% rated thermal power (RTP) throughout the report
Reoort Details
      period, except for routine testing activities.
Summary of Plant Status
      Unit 2 began the report period at 100% RTP. On January 5, power was
Unit 1 operated at 100% rated thermal power (RTP) throughout the report
      reduced to about 93.5% RTP due to a feedwater heater isolation. Power
period, except for routine testing activities.
      was returned to 100% RTP on the same day and operated at this power level
Unit 2 began the report period at 100% RTP. On January 5, power was
      throughout the remainder of the report period, except for routine testing
reduced to about 93.5% RTP due to a feedwater heater isolation.
      activities.
Power
                                    I. Operations
was returned to 100% RTP on the same day and operated at this power level
      01.   Conduct of Operations
throughout the remainder of the report period, except for routine testing
      01.1 General Comments (71707)
activities.
                                                                                  i
I. Operations
            The inspectors conducted frequent reviews of ongoing plant
01.
            operations. In general, the conduct of operations was
Conduct of Operations
            professional and safety-conscious: s
01.1 General Comments (71707)
            are detailed in the sections below. pecific events and observation   ;
i
      01.2 Control Room Panel Walkdown
The inspectors conducted frequent reviews of ongoing plant
      a.   Insoection Scooe (71707)
operations.
            On January 10. the ins)ectors conducted a control room panel
In general, the conduct of operations was
            walkdown of Unit 2. T1e walkdown included safety- and
are detailed in the sections below. pecific events and observation
            non-safety-related equipment valve lineups, switch positions and     i
professional and safety-conscious: s
            process instrument indications.
01.2 Control Room Panel Walkdown
      b.   Observations and Findinos
a.
                                                                                  l
Insoection Scooe (71707)
            The inspectors observed that both keepfill pumps on the B loop of     i
On January 10. the ins)ectors conducted a control room panel
            Residual Heat Removal System (RHR) were in service.   One control   i
walkdown of Unit 2.
            switch was in run and the standby pump control switch was in auto.
T1e walkdown included safety- and
            This observation was brought to the attention of the control board     ;
non-safety-related equipment valve lineups, switch positions and
                                                                                  '
i
            operator. The operator indicated that the B loop of RHR had been
process instrument indications.
            in service for torus cooling during previous surveillance
b.
            activities and had been secured earlier that day, following the
Observations and Findinos
            completion of the surveillance activities. Tne operator indicated
The inspectors observed that both keepfill pumps on the B loop of
            that securing the RHR pump may have caused a small pressure surge       ,
Residual Heat Removal System (RHR) were in service.
            that initiated the automatic start of the standby keepfill pump.     !
One control
            The operator secured the standby pump and system pressure remained
i
            satisfactory.
switch was in run and the standby pump control switch was in auto.
            The inspectors also observed that the by) ass selector switch for
This observation was brought to the attention of the control board
            the A Source Range Monitor (SRM) was in )ypass.   This was brought
'
            to the attention of the control board operator.   The operator
operator.
                                                                      Enclosure 2 I
The operator indicated that the B loop of RHR had been
                                                                                    l
in service for torus cooling during previous surveillance
activities and had been secured earlier that day, following the
completion of the surveillance activities. Tne operator indicated
that securing the RHR pump may have caused a small pressure surge
,
!
that initiated the automatic start of the standby keepfill pump.
The operator secured the standby pump and system pressure remained
satisfactory.
The inspectors also observed that the by) ass selector switch for
the A Source Range Monitor (SRM) was in )ypass.
This was brought
to the attention of the control board operator.
The operator
Enclosure 2


                            .-     _   _ _ .
.-
                                        _          . -   - - - .             -           . - - - . . .
_
    .
_ _ .
  .
. -
                                                                                                            !
- - - .
                                                2
-
            stated that the A SRM instrument cabinet had been removed from the
. - - - . .
            control room panel on January 9. for Instrumentation and Control
.
          ~( I&C) work activities. The SRM instrument cabinet had been
_
            replaced on the previous shift The SRM bypass selector switch
.
            had not been returned to normal.                                                             l
.
            The inspectors brought these deficiencies to the attention of
2
            operations' management for resolution.               Management's expectations
stated that the A SRM instrument cabinet had been removed from the
            are in part, that the operators walkdown the control room front
control room panel on January 9. for Instrumentation and Control
            panels once per hour and back panels once per two hours and look
~ I&C) work activities. The SRM instrument cabinet had been
            for changing trends and incorrect switch positions.                                           ,
(
                                                                                                          !
replaced on the previous shift
      c.   Conclusions
The SRM bypass selector switch
            The inspectors did not consider these deficiencies to be an
had not been returned to normal.
            immediate concern for plant safety. The inspectors concluded that
l
            control room operators demonstrated a lack of attention to detail
The inspectors brought these deficiencies to the attention of
            during control room panel walkdowns. Operators failed to observe                             *
operations' management for resolution.
            an incorrect switch position and a keepfill pump that had
Management's expectations
            automatically started.
are in part, that the operators walkdown the control room front
      05   Operator Training and Qualification                                                           ;
panels once per hour and back panels once per two hours and look
                                                                                                          !
for changing trends and incorrect switch positions.
      05.1 Review of ooerator "Just in Time" Trainina
,
                                                                                                          '
!
.      a.    Insoection Scooe (71707)
c.
            A new training initiative, entitled "Just in Time" training
Conclusions
The inspectors did not consider these deficiencies to be an
immediate concern for plant safety.
The inspectors concluded that
control room operators demonstrated a lack of attention to detail
during control room panel walkdowns. Operators failed to observe
*
an incorrect switch position and a keepfill pump that had
automatically started.
05
Operator Training and Qualification
;
!
!
            commenced to address previous problems associated with activities
05.1 Review of ooerator "Just in Time" Trainina
i           that would affect operators. Operations' management began "Just
'
            in Time" training sessions for 03erators due to previous problems
a.
Insoection Scooe (71707)
.
A new training initiative, entitled "Just in Time" training
!
commenced to address previous problems associated with activities
i
that would affect operators.
Operations' management began "Just
in Time" training sessions for 03erators due to previous problems
!
with reverse power trips of the EDGs during surveillance
,
,
          with reverse power trips of the EDGs during surveillance                                      !
activities.
On December 26. the inspectors observed two sessions
!
i
i
            activities.    On December 26. the inspectors observed two sessions                          !
of "Just In Time" training for EDG manipulations during
            of "Just In Time" training for EDG manipulations during
i
i           surveillance activities.                                                                     l
surveillance activities.
      b. Observations and Findinas                                                                     :
l
          The inspectors observed that the "Just in Time" training was
b.
          conducted on the plant simulator. One session provided an
Observations and Findinas
.          o)erator the opportunity to review the procedure and manipulate                               1
:
:          t1e switches                                                                                !
The inspectors observed that the "Just in Time" training was
          surveillance. prior Thetoother
conducted on the plant simulator.
                                    performing
One session provided an
                                            trainingansession
o)erator the opportunity to review the procedure and manipulate
                                                        inplant provided
.
                                                                    Unit 2 EDG
1
                                                                            a different                 ,
!
          operator the same opportunity prior to performing a Unit 1 EDG                               !
surveillance. prior to performing an inplant Unit 2 EDG
t1e switches
:
The other training session provided a different
,
operator the same opportunity prior to performing a Unit 1 EDG
!
surveillance.
!
;
;
          surveillance.                                                                                !
i
                                                                                                        i
The inspectors observed that the training sessions were self
            The inspectors observed that the training sessions were self
directed by the operators and required very little instructor
          directed by the operators and required very little instructor
assistance. The operators reviewed the apolicable procedures and
          assistance. The operators reviewed the apolicable procedures and                             ,
,
-
-
                                                                                                        :
:
1
1
                                                                                        Enclosure 2     ;
Enclosure 2
                                                                                                        l
;
                                                                                                        :
l
:
'
'
                                                -                   -           . _ . -
-
-
.
. -


  .
    -
.
.
                                                                                \
\\
                                                                                l
-
                                        3
.
            performed the necessary manipulations to complete the               ;
3
            surveillances.                                                       ;
performed the necessary manipulations to complete the
                                                                                ;
;
            The inspectors discussed with operations' management if training
surveillances.
            on the simulator, which is modeled after Unit 2. may present
;
            additional challenges to operator performance when performing
The inspectors discussed with operations' management if training
            Unit 1 activities.   Operations' management indicated no and
on the simulator, which is modeled after Unit 2. may present
            stated that, even though the simulator was modeled for Unit 2 any
additional challenges to operator performance when performing
            switch manipulation practice would be of benefit to the operators.
Unit 1 activities.
      c.   Conclusions
Operations' management indicated no and
            The inspectors concluded that operations' management was proactive
stated that, even though the simulator was modeled for Unit 2 any
            with respect to providing operators training to correct or prevent
switch manipulation practice would be of benefit to the operators.
            some deficiencies by the "Just In Time" training. The inspectors
c.
            observed that the "Just in Time" training was not a formal or
Conclusions
            proceduralized process; however, operators or super isors may
The inspectors concluded that operations' management was proactive
            request training at their discretion.
with respect to providing operators training to correct or prevent
      05.2 00erator Fire Briaade trainina and Qualification
some deficiencies by the "Just In Time" training.
      a.   Inspection Scooe 71707
The inspectors
            The inspectors reviewed fire training requirements and
observed that the "Just in Time" training was not a formal or
            qualifications for a shift of operations aersonnel. The review
proceduralized process; however, operators or super isors may
            was conducted for fire fighters and fire ]rigade leaders.
request training at their discretion.
      b.   Observations and Findinas
05.2 00erator Fire Briaade trainina and Qualification
            The inspectors reviewed the licensee's Training Records and
a.
            Qualification System Matrix Report and confirmed that operators on
Inspection Scooe 71707
            shift were indicated as qualified for their fire fighting
The inspectors reviewed fire training requirements and
            positions. The inspectors also verified that the operators had
qualifications for a shift of operations aersonnel. The review
            successfully completed the required initial and requalification
was conducted for fire fighters and fire ]rigade leaders.
            training to maintain their qualifications.
b.
            The inspectors also verified that corrective lenses were available
Observations and Findinas
            in the control room for operators' use during emergencies that may
The inspectors reviewed the licensee's Training Records and
            require SCBAs to be worn. The inspectors observed that six
Qualification System Matrix Report and confirmed that operators on
            operators that required corrective lenses license restriction did
shift were indicated as qualified for their fire fighting
            not have corrective eye glasses stored in the designated storage
positions.
            location in the control room. The inspectors were informed by
The inspectors also verified that the operators had
            operations supervision that the six operators wore contact lenses
successfully completed the required initial and requalification
            instead of eye glasses. The inspectors reviewed ap)licable
training to maintain their qualifications.
            procedures that dealt with wearing contact lenses w111e wearing a
The inspectors also verified that corrective lenses were available
            SCBA and concluded that the procedures and training were adequate.
in the control room for operators' use during emergencies that may
                                                                    Enclosure 2
require SCBAs to be worn.
The inspectors observed that six
operators that required corrective lenses license restriction did
not have corrective eye glasses stored in the designated storage
location in the control room. The inspectors were informed by
operations supervision that the six operators wore contact lenses
instead of eye glasses.
The inspectors reviewed ap)licable
procedures that dealt with wearing contact lenses w111e wearing a
SCBA and concluded that the procedures and training were adequate.
Enclosure 2


        -
-
                                                                                          :
:
                                                                                          '
'
          .
.
                                                                                          I
                                                4
                                                                                          l
            c.  Conclusions                                                            i
4
4
                  The inspectors concluded that the shift of operators reviewed for       :
l
                  fire fighting and fire brigade leader training and qualifications
c.
                  were trained and qualified for their assigned position.         .       :
Conclusions
  .
i
                  Operators' corrective lenses for use while wearing a SCBA. during
4
  i              control room emergencies, were readily available in the control         !
The inspectors concluded that the shift of operators reviewed for
  i               room.                                                                   .
:
                                                                                          3
fire fighting and fire brigade leader training and qualifications
            07   Quality Assurance in Operations                                         l
were trained and qualified for their assigned position.
.           07.1 Licensee Self-Assessment Activities (40500)
.
            a.   Insoection Scooe 40500                                                 i
:
  ;
.
j                 The inspectors reviewed two licensee self assessments and followup
Operators' corrective lenses for use while wearing a SCBA. during
                  actions and a new procedure for Team Observations.
control room emergencies, were readily available in the control
;
!
.            b.   Observations and Findinas                                                 '
i
i
room.
.
3
07
Quality Assurance in Operations
.
07.1 Licensee Self-Assessment Activities (40500)
a.
Insoection Scooe 40500
i
;
j
The inspectors reviewed two licensee self assessments and followup
actions and a new procedure for Team Observations.
;
b.
Observations and Findinas
'
.
1
The inspectors reviewed a self assessment for operations
,
activities with respect to reactivity controls.
Following
1
1
                  The inspectors reviewed a self assessment for operations
operator errors during refueling activities, control rod movement
                  activities with respect to reactivity controls. Following
'
                                                                                            ,
{
                                                                                            !
errors, and inattention to detail, the licensee initiated a self
1                operator errors during refueling activities, control rod movement       '
;
{                 errors, and inattention to detail, the licensee initiated a self
assessment to identify root causes and recommend corrective
;                 assessment to identify root causes and recommend corrective
' -
'-
actions.
                  actions.                                                                 l
l
                  The inspectors reviewed the licensee's completed actions with             l
The inspectors reviewed the licensee's completed actions with
,                respect to implementing the recommendations. The inspectors             ,
respect to implementing the recommendations.
                  observed that 7 of 20 recommendations were not completed.
The inspectors
.                However, the licensee's documentation indicated that the remaining
,
i                 open items would be com eted prior to the Unit 2 refueling outage       '
,
!                 scheduled for March 199
observed that 7 of 20 recommendations were not completed.
                                                                                          '
However, the licensee's documentation indicated that the remaining
!                The inspectors reviewed an operations department self assessment
.
.                completed on about September 26, 1996 that focused on identifying
i
'                needed enhancements and generating corrective action
open items would be com eted prior to the Unit 2 refueling outage
                  recommendations aimed at hel)ing the department achieve its goal
'
:                 of excellent performance. T1e assessment was conducted at the           ,
!
scheduled for March 199
!
The inspectors reviewed an operations department self assessment
'
completed on about September 26, 1996 that focused on identifying
.
needed enhancements and generating corrective action
'
recommendations aimed at hel)ing the department achieve its goal
:
of excellent performance.
T1e assessment was conducted at the
,
request of operations' management and conducted by personnel both
j
.
within and outside the parent organization.
l
The inspectors observed that the assessment included safety focus.
management involvement, problem identification, problem
:
resolution, quality of operations, programs and procedures, and
:
operations efficiencies.
The inspectors also observed that the
i
assessment provided specific observations and recommendations.
'
;
.
The inspectors also reviewed procedure DI-0PS-59-0896N:
Team
,
Observations. Revision 0, and observed that the procedure provided
i
:
Enclosure 2
;
I
;
t
.
.
                  request of operations' management and conducted by personnel both      j
                  within and outside the parent organization.                            l
                  The inspectors observed that the assessment included safety focus.      !
                  management involvement, problem identification, problem                :
                  resolution, quality of operations, programs and procedures, and        :
                  operations efficiencies. The inspectors also observed that the          i
                  assessment provided specific observations and recommendations.
                                                                                          '
.
.
                                                                                          ;
. .
,                The inspectors also reviewed procedure DI-0PS-59-0896N: Team
-l
                  Observations. Revision 0, and observed that the procedure provided    i
..
                                                                                          :
--
                                                                            Enclosure 2
-
                                                                                        ;
,,
                                                                                        I
_
;                                                                                        t
-
    ..                  --  -                                                        -l


  ,- - . . --       .       . - - - - -. - - - - . . - , _ - - . - - . . _ - . - -
,-
4                                                                                                                     t
- . .
                                                                                                                      *
--
                                                                  5
.
                                                                                                                      i
. - - - - -. - - - - . . - , _ - - . - - . . _ - . - -
                                                                                                                      '
4
                a means of observing and reinforcing the operations department's
t
                expectations by performing supervisory and peer evaluations on                                       ;
*
                routine tasks. Checklists for specific activities were included                                       i
5
                and contained a method of identifying whether or not the                                             j
i
                expectations were met.                                                                               ,
a means of observing and reinforcing the operations department's
                                                                                                                      3
'
                The inspectors reviewed some completed observations, checklists.                                     !
expectations by performing supervisory and peer evaluations on
                and comments and discussed them with operation's management.
;
                Operations' management stated that the process was still being
routine tasks.
                improved and a revision of the procedure was being developed.
Checklists for specific activities were included
                                                                                                                      r
i
              c. Conclusions                                                                                           >
and contained a method of identifying whether or not the
                The inspectors concluded that the operations department                                               i
j
                demonstrated a commitment to self assessment and a desire for                                         ;
expectations were met.
                continued improvement. Although some corrective recommendations                                       l
,
                were not com)leted, they were under development and the completed                                     i
3
                items were t1orough and comprehensive. The self assessments were                                     j
The inspectors reviewed some completed observations, checklists.
                conducted by knowledgeable personnel.                                                                 i
!
                                                                                                                      i
and comments and discussed them with operation's management.
          08   Miscellaneous Operations Issues                                                                       i
Operations' management stated that the process was still being
          08.1 Cold Weather Followuo and Walkdown                                                                     -
improved and a revision of the procedure was being developed.
              a. Insoection Scooe (71714)(92901)                                                                       l
r
                The inspectors performed a walkdown of systems and plant
c.
                structures during hard freeze warnings.
Conclusions
              b. Observation and Findinas                                                                             ,
>
                                                                                                                      :
The inspectors concluded that the operations department
                The inspectors observed the following during the walkdown:                                           l
i
                                                                                                                      !
demonstrated a commitment to self assessment and a desire for
                -
;
                    Two of the four wall manual louvers in the Fire Pump House were                                   ;
continued improvement. Although some corrective recommendations
                    not closed completely. The louvers were o
l
                      inch. The manual roof vent was also open. pen approximately one
were not com)leted, they were under development and the completed
                -
i
                    Three heat trace indicating lights were not illuminated. Two                                     >
items were t1orough and comprehensive. The self assessments were
                    were on the fire protection water system and the other was on                                     i
j
                    the cooling water to the IB EDG.
conducted by knowledgeable personnel.
                                                                                                                      '
i
                -
i
                    Several automatic louvers in the EDG rooms were not completely
08
                    closed as required.                                                                               ,
Miscellaneous Operations Issues
                The inspectors found from that some deficiencies still existed                                       !
i
                that had been previously observed as documented in                                                     ;
08.1 Cold Weather Followuo and Walkdown
                IR 50-321. 366/96-14.                                                                                 l
-
                                                                                                                        l
a.
                Following a hard freeze warning on about December 21. Plant                                           !
Insoection Scooe (71714)(92901)
                Equipment Operators (PE0) could not get the up-river or the down-                                     '
l
                                                                                            Enclosure 2                 ,
The inspectors performed a walkdown of systems and plant
                                                                                                                        l
structures during hard freeze warnings.
                                                                                                                        ,
b.
                                                                                    . _ _ _   ,.m . ___ _ _ _. . _ _ _
Observation and Findinas
,
:
The inspectors observed the following during the walkdown:
l
!
-
Two of the four wall manual louvers in the Fire Pump House were
;
not closed completely. The louvers were o
The manual roof vent was also open. pen approximately one
inch.
-
Three heat trace indicating lights were not illuminated. Two
>
were on the fire protection water system and the other was on
i
the cooling water to the IB EDG.
'
Several automatic louvers in the EDG rooms were not completely
-
closed as required.
,
The inspectors found from that some deficiencies still existed
!
that had been previously observed as documented in
IR 50-321. 366/96-14.
l
Following a hard freeze warning on about December 21. Plant
Equipment Operators (PE0) could not get the up-river or the down-
'
Enclosure 2
,
l
,
. _ _ _
,.m
. ___ _ _
_.
.


  . . _ - . - - .   -- .           __ -     . - . . . - - - - -               - - .       . - - - . -
. . _ - . - - .
                                                                                                          !
-- .
            .
__
                                                                                                          l
-
  *
. - . . . - - - - -
                                                                                                          !
- - .
                                                                                                          ;
. - - - . -
!
l
.
*
!
;
!.
!.
-
-
                                                                                                          '
6
                                                                    6
'
.                          river traveling water screens to operate. Subsequent trouble                   i
river traveling water screens to operate.
!                         shooting by maintenance personnel identified that the pressure                 ,
Subsequent trouble
                          switches for both screens had frozen. The inspectors observed the               i
i
                                                                                                          '
.
                          pressure switch installations and observed that the sensing lines
!
                          to the switches were heat traced, but a problem existed in that                 #
shooting by maintenance personnel identified that the pressure
                          switches were not heat traced or insulated in order to read their               ;
,
                          indication. Maintenance personnel corrected this problem and
switches for both screens had frozen. The inspectors observed the
                          later enclosed the switches with insulating material, installed
i
                          heat lamas and directed the lamps toward the pressure switches. A
pressure switch installations and observed that the sensing lines
                          design clange was initiated to make permanent repairs.
'
                          The inspectors were informed that operations personnel had tested               !
to the switches were heat traced, but a problem existed in that
                          the traveling screens due to information received from industry                 l
#
                          experience. Freezing problems with traveling screens had been                   i
switches were not heat traced or insulated in order to read their
                          identified at other sites.                                                     l
indication. Maintenance personnel corrected this problem and
                                                                                                          t
;
                          The inspectors found from the reviews and discussions with                     l
later enclosed the switches with insulating material, installed
                          licensee personnel that the traveling water screen system for both
heat lamas and directed the lamps toward the pressure switches. A
                          units would not operate in manual or automatic due to the pressure
design clange was initiated to make permanent repairs.
                          switch problem. As a result, the support systems affecting plant               ,
The inspectors were informed that operations personnel had tested
                          safety systems, such as Plant Service Water (PSW) and Residual
!
                          Heat Removal Service Water "lHRSW). were not available during this             !
the traveling screens due to information received from industry
                          cold weather condition. The licensee's prompt corrective actions
l
                          restored the function of the pressure switches. The affected
experience.
                          plant safety systems would have performed their required                       >
Freezing problems with traveling screens had been
                          functions.
i
                  c.     Conclusions
identified at other sites.
                          The inspectors concluded that the deficiencies obser ved during the             i
l
                          walk downs were not significant for the existing outside                         ;
t
                          temperatures and the cleanliness of the river water and river                   i
The inspectors found from the reviews and discussions with
                          level at the time of the walk downs. Maintenance and operations                 l
l
                          personnel failed to identify that portions of the system were
licensee personnel that the traveling water screen system for both
                          vulnerable to cold weather conditions during their system checks
units would not operate in manual or automatic due to the pressure
                          and cold weather preparations. Engineering personnel failed to
switch problem. As a result, the support systems affecting plant
                          identify that the design and system configuration did not
,
                          adequately protect system components from cold weather conditions.
safety systems, such as Plant Service Water (PSW) and Residual
                          The failure of the traveling water screen system to operate during
Heat Removal Service Water "lHRSW). were not available during this
                          cold weather conditions is identified as a significant weakness in
!
                          the area of engineering.
cold weather condition. The licensee's prompt corrective actions
                                                                                                            :
restored the function of the pressure switches. The affected
                                                                                        Enclosure 2
plant safety systems would have performed their required
                                                                                                            l
>
                                                                                                            l
functions.
                                                                                                            :
c.
                                                                                                            !
Conclusions
The inspectors concluded that the deficiencies obser ved during the
i
walk downs were not significant for the existing outside
temperatures and the cleanliness of the river water and river
i
level at the time of the walk downs.
Maintenance and operations
personnel failed to identify that portions of the system were
vulnerable to cold weather conditions during their system checks
and cold weather preparations.
Engineering personnel failed to
identify that the design and system configuration did not
adequately protect system components from cold weather conditions.
The failure of the traveling water screen system to operate during
cold weather conditions is identified as a significant weakness in
the area of engineering.
Enclosure 2
l


_ ...   - . - - - . . - . - . - .. .-                           _ -     ..   --           -   - - - _ . ---             -.
_ ...
                                                                                                                                  l
- . - - - . . - . - . - .. .-
      *
_
    .
-
                                                                                                                                  r
..
                                                                                                                                  !
--
                                                                      7
-
                                                                                                                                  l
- - - _ . ---
                                                            II. Maintenance
-.
                          M1         Conduct of Maintenance                                                                     !
l
                                *
*
                                                                                                                                  !
.
                          M1.1 General Comments                                                                                 ;
r
                                                                                                                                  ;
7
                              a.       Insoection Scooe (62707)                                                                 j
II. Maintenance
                                      The inspectors observed all or portions of the following work                             !
M1
                                      activities *                                                                               I
Conduct of Maintenance
                                                                                                                                  \
!
                                        -
!
                                            MWO 1-96-4722:   Electrically backseat RCIC Inboard                                   J
*
                                                                    Isolation Valve 1E51-F007
M1.1 General Comments
                                        -
;
                                            MWO 1-96-4362:   Electrically backseat RWCU Inboard
;
                                                                    Isolation Valve 1G31-F001                                   1
a.
                                        -
Insoection Scooe (62707)
                                            MWO 2-96-3361: Repair 1B EDG Auto Voltage Regulator                                   i
j
                                        -
The inspectors observed all or portions of the following work
                                            MWO 2-96-0042: Repair Unit 2 RCIC EGM Control Box
!
                                        -
activities *
                                            MWO 2-96-2976: Repair Unit 2 RCIC Data Input to DAAS
I
                                        -
\\
                                            MWO 1-97-0066: Investigate Tripping of 1A SLC Pump
J
                                        -
-
                                            MWO 1-97-0071: Replace Overload Heaters in 1A SLC Pump
MWO 1-96-4722:
                                        -
Electrically backseat RCIC Inboard
                                            MWO 1-97-0092: Replace Overload Relay for 1A SLC Pump
Isolation Valve 1E51-F007
                              b.       Observations and Findinas
MWO 1-96-4362:
                                      The inspectors found that the work was performed in accordance
Electrically backseat RWCU Inboard
                                      with actively used work packages. Appro)riate post modification
-
                                      and maintenance tests were performed. Tlese tests consisted of
Isolation Valve 1G31-F001
                                      operating the equipment following the completion of work
-
                                      activities.
MWO 2-96-3361: Repair 1B EDG Auto Voltage Regulator
                                      Additional inspector observations are documented in Sections M1.2
i
                                      and M1.3.
-
                          M1 -. 2 Reoairs to 1B EDG Automatic Voltaae Reaulator
MWO 2-96-0042: Repair Unit 2 RCIC EGM Control Box
                            a.       Insoection Scone (62707)                                                                   !
MWO 2-96-2976:
                                                                                                                                  l
Repair Unit 2 RCIC Data Input to DAAS
                                      The inspectors observed work activities performed on the IB                               l
-
                                      Emergency Diesel Generator (EDG) automatic voltage regulator under                         ;
MWO 1-97-0066:
                                      Maintenance Work Order (MWO) 2-96-3361. The inspectors discussed                           !
Investigate Tripping of 1A SLC Pump
                                      the activities with maintenance, engineering and operations                               !
-
                                      personnel.
-
                            b.       Observations and Findinas
MWO 1-97-0071:
                                      The inspectors were informed that while performing 3rocedure                               l
Replace Overload Heaters in 1A SLC Pump
                                      34SV-R43-002-2S: Diesel Generator IB Monthly Test
-
                                                                                                                                  '
MWO 1-97-0092:
                                                                                                          Rev.18, with
Replace Overload Relay for 1A SLC Pump
                                      voltage regulation in automatic control and the voltage at 4120
b.
                                      volts alternating current (VAC), the voltage could not be adjusted
Observations and Findinas
                                                                                                                  Enclosure 2
The inspectors found that the work was performed in accordance
-                                           .   -                       .     .     . - - _ , . .                     -
with actively used work packages. Appro)riate post modification
and maintenance tests were performed. Tlese tests consisted of
operating the equipment following the completion of work
activities.
Additional inspector observations are documented in Sections M1.2
and M1.3.
M1 -. 2 Reoairs to 1B EDG Automatic Voltaae Reaulator
a.
Insoection Scone (62707)
l
The inspectors observed work activities performed on the IB
Emergency Diesel Generator (EDG) automatic voltage regulator under
Maintenance Work Order (MWO) 2-96-3361. The inspectors discussed
the activities with maintenance, engineering and operations
personnel.
b.
Observations and Findinas
The inspectors were informed that while performing 3rocedure
34SV-R43-002-2S: Diesel Generator IB Monthly Test
Rev.18, with
'
voltage regulation in automatic control and the voltage at 4120
volts alternating current (VAC), the voltage could not be adjusted
Enclosure 2
-
.
-
.
.
. - - _ , . .
-


                                                                            -
-
.                                                                             I
.
                                                                              i
i
                                                                              1
1
                                    8                                         i
8
        to the required 4160 VAC. The automatic voltage adjustment must'
i
        be performed at the local panel due to the design of the system.       l
to the required 4160 VAC. The automatic voltage adjustment must'
        Troubleshooting activities discovered defective diodes in the         :
be performed at the local panel due to the design of the system.
        direct current drive motor circuit of the voltage regulator. The       !
l
        motor positions the automatic regulator rheostat which sets the
Troubleshooting activities discovered defective diodes in the
        voltage level for automatic control. The inspectors discussed the
:
        failure of the diodes with engineering personnel and were informed
direct current drive motor circuit of the voltage regulator. The
                                                                              '
!
        that the motor and rheostat were seldom exercised and this may         i
motor positions the automatic regulator rheostat which sets the
        have contributed to the failure. The system engineer indicated
voltage level for automatic control. The inspectors discussed the
                                                                                '
failure of the diodes with engineering personnel and were informed
      that a recommendation to exercise the motor and rheostat more
'
      often would be made.                                                     ,
that the motor and rheostat were seldom exercised and this may
                                                                                ,
i
        During the repair activities. the inspectors observed that the new     l
have contributed to the failure.
      diodes were installed by craft personnel using applicable               l
The system engineer indicated
      procedures with supervisory and engineering oversight. Subsequent       i
'
      to the repair, a new motor-rheostat unit was installed and the           l
that a recommendation to exercise the motor and rheostat more
        repaired unit was returned to the warehouse as a spare.               ]
often would be made.
      The inspectors were informed by engineering that the EDG would
,
      have controlled the voltage in automatic at 4120 VAC instead of
,
      4160 VAC and the difference in voltage was not enough to affect
During the repair activities. the inspectors observed that the new
      safety-related loads.
diodes were installed by craft personnel using applicable
  c. Conclusion
procedures with supervisory and engineering oversight. Subsequent
      Maintenance activities observed were generally thorough and
i
      professional. Supervisory and engineering oversight were evident.
to the repair, a new motor-rheostat unit was installed and the
      The inspectors concluded that the work activities and the review
repaired unit was returned to the warehouse as a spare.
      by the sy'. tem engineer for the IB EDG voltage regulator were
]
      thorough and performed in accordance with applicable procedures.
The inspectors were informed by engineering that the EDG would
      The inspectors also concluded that the EDG was capable of
have controlled the voltage in automatic at 4120 VAC instead of
      performing the required safety functions.
4160 VAC and the difference in voltage was not enough to affect
  M1.3 Reoairs to Unit 2 Reactor Core Isolation Coolino (RCIC) Turbine
safety-related loads.
      Soeed Control
c.
  a.   Insoection Scone (62707)
Conclusion
      The inspectors reviewed the results of the maintenance activities
Maintenance activities observed were generally thorough and
      and observed the post maintenance test of the Unit 2 RCIC turbine.
professional.
      The system had been declared inoperable due to speed control
Supervisory and engineering oversight were evident.
      problems.
The inspectors concluded that the work activities and the review
  b. Observations and Findinos                                               I
by the sy'. tem engineer for the IB EDG voltage regulator were
      The activities were performed under MW0s 2-96-0042 and 2-96-2976.
thorough and performed in accordance with applicable procedures.
      and ap)licable procedures. Trouble shooting activities indicated
The inspectors also concluded that the EDG was capable of
      that tie electronic governor motor (EGM) was defective. The EGM           l
performing the required safety functions.
      Control Box was replaced and the RCIC was satisfactorily tested.         I
M1.3 Reoairs to Unit 2 Reactor Core Isolation Coolino (RCIC) Turbine
                                                                                l
Soeed Control
                                                                Enclosure 2   i
a.
Insoection Scone (62707)
The inspectors reviewed the results of the maintenance activities
and observed the post maintenance test of the Unit 2 RCIC turbine.
The system had been declared inoperable due to speed control
problems.
b.
Observations and Findinos
The activities were performed under MW0s 2-96-0042 and 2-96-2976.
and ap)licable procedures.
Trouble shooting activities indicated
that tie electronic governor motor (EGM) was defective. The EGM
Control Box was replaced and the RCIC was satisfactorily tested.
l
i
Enclosure 2


  .
    *
.
.
                                        9
*
          The defective electronic governor was bench tested and confirmed
.
          that the trouble shooting findings were correct. Inspector
9
          observations on the Unit 2 RCIC post maintenance and operability
The defective electronic governor was bench tested and confirmed
            testing are documented in Section M3.3 of this report.
that the trouble shooting findings were correct.
      c. Conclusions
Inspector
          Maintenance activities observed were generally thorough and
observations on the Unit 2 RCIC post maintenance and operability
          professional. Supervisory and engineering oversight were evident.
testing are documented in Section M3.3 of this report.
          The ins)ectors concluded that the maintenance activities on the
c.
          Unit 2 RCIC identified and corrected the 3roblem with the
Conclusions
            fluctuations in turbine speed control. T1e two reversed wires
Maintenance activities observed were generally thorough and
          discovered did not affect system operability but demonstrated a
professional. Supervisory and engineering oversight were evident.
            lack of attention to detail.
The ins)ectors concluded that the maintenance activities on the
      M1.4 Electrical Maintenance Imolementation
Unit 2 RCIC identified and corrected the 3roblem with the
      a.   Insoection Scooe (62700)
fluctuations in turbine speed control. T1e two reversed wires
          To evaluate electrical maintenance implementation as it relates to
discovered did not affect system operability but demonstrated a
          motor generator (MG) sets and switchyard equipment, the inspectors   ,
lack of attention to detail.
          conducted: walkdown inspections of the Reactor Protection System
M1.4 Electrical Maintenance Imolementation
            (RPS) and Reactor Recirculation System (RR) MG set rooms and
a.
          selected areas of the switchyards and the switchyard control         !
Insoection Scooe (62700)
          house; and reviews of equipment manufacturers' technical manuals.     l
To evaluate electrical maintenance implementation as it relates to
          re)etitive task records, maintenance records, and oil analysis and
motor generator (MG) sets and switchyard equipment, the inspectors
          vi) ration test data. The inspectors compared the equipment
,
          manufacturers' maintenance recommendations with the licensee's
conducted: walkdown inspections of the Reactor Protection System
          maintenance program for both scope and periodicity.
(RPS) and Reactor Recirculation System (RR) MG set rooms and
      b.   Observations and Findinas
selected areas of the switchyards and the switchyard control
          Reactor Protection System and Reactor Recirculation System MG Sets
!
          Housekeeping was good with the following exceptions:
house; and reviews of equipment manufacturers' technical manuals.
          o   A number of structural fasteners were missing from control
l
                panels. The concern was that the missing fasteners could
re)etitive task records, maintenance records, and oil analysis and
                abrogate the seismic qualification of the pariels.
vi) ration test data.
          e   The closure devices on a number of panel doors were not secured
The inspectors compared the equipment
                such that the weather stripping was compressed. The concern
manufacturers' maintenance recommendations with the licensee's
                was that the improper sealing of the panels could abrogate the
maintenance program for both scope and periodicity.
                environmental qualification.
b.
          e   Metal shavings (probably the debris left from drilling) and
Observations and Findinas
                miscellaneous fasteners were found adrift inside control
Reactor Protection System and Reactor Recirculation System MG Sets
                panels. Leaving loose conductive material in electrical panels
Housekeeping was good with the following exceptions:
                was identified as a poor work practice control with the
o
                                                                    Enclosure 2
A number of structural fasteners were missing from control
panels.
The concern was that the missing fasteners could
abrogate the seismic qualification of the pariels.
e
The closure devices on a number of panel doors were not secured
such that the weather stripping was compressed.
The concern
was that the improper sealing of the panels could abrogate the
environmental qualification.
e
Metal shavings (probably the debris left from drilling) and
miscellaneous fasteners were found adrift inside control
panels.
Leaving loose conductive material in electrical panels
was identified as a poor work practice control with the
Enclosure 2


                                                                      _ _ _ _     . _ . _
.
      .
_ _ _ _
        ,
. _ . _
  .
,
    ,
.
                                        10
,
                potential of shorting out components.   The fasteners were
10
                removed by the licensee,
potential of shorting out components.
          e   The Reactor Recirculation System MG set oil circulation systems
The fasteners were
                leak. To address this issue, the licensee conducts daily wipe
removed by the licensee,
                downs and was actively pursuing a permanent repair.
e
          There was a number of areas where the liccnsee's repetitive
The Reactor Recirculation System MG set oil circulation systems
          preventive maintenance program was not consistent with the                       <
leak.
          equipment manufacturer's recommendations. The licensee was unable             )
To address this issue, the licensee conducts daily wipe
          to provide documented justifications for the differences.                       i
downs and was actively pursuing a permanent repair.
          However, the licensee was able to provide anecdotal information               j
There was a number of areas where the liccnsee's repetitive
preventive maintenance program was not consistent with the
<
equipment manufacturer's recommendations. The licensee was unable
)
to provide documented justifications for the differences.
i
However, the licensee was able to provide anecdotal information
j
remembered by maintenance personnel that supported the deviations.
>
>
          remembered by maintenance personnel that supported the deviations.
Records, examined by the inspectors. reflected that repetitive
          Records, examined by the inspectors. reflected that repetitive
:
:         preventive maintenance activities were completed within the
preventive maintenance activities were completed within the
;         scheduled time period.
;
I         Records reflect that the repetitive preventive maintenance program             !
scheduled time period.
                                                                                            '
I
          had been effective as few repetitive corrective maintenance
Records reflect that the repetitive preventive maintenance program
!
'
had been effective as few repetitive corrective maintenance
i
activities were required.
l
i
i
          activities were required.                                                      l
Switchyards
i          Switchyards
;
;
          Maintenance in the switchyards was performed by Georgia Power
Maintenance in the switchyards was performed by Georgia Power
          Company Transmission Maintenance Center with procedures issued by             l
Company Transmission Maintenance Center with procedures issued by
l         the Transmission Operation and Maintenance Manager. Some                       *
l
j         surveillances were performed by Plant Hatch Operations Department             l
l
          personnel.
the Transmission Operation and Maintenance Manager.
:         Ins)ection of housekeeping and material condition revealed a                   I
Some
*
j
surveillances were performed by Plant Hatch Operations Department
l
personnel.
:
Ins)ection of housekeeping and material condition revealed a
I
num)er of items that needed attention.
Protective coatings on
4
4
          num)er of items that needed attention. Protective coatings on
l
l          exterior equipment had deteriorated, as evidenced by many areas of             )
exterior equipment had deteriorated, as evidenced by many areas of
l         rust and missing closure fasteners. Inside the switch house, the
)
          inspectors noted un-taped spare electrical leads in the back board
l
i         area, trash, and evidence of feline habitation.     Conductive
rust and missing closure fasteners.
Inside the switch house, the
inspectors noted un-taped spare electrical leads in the back board
i
area, trash, and evidence of feline habitation.
Conductive
material (metal shavings and fasteners) was found in both exterior
l
<
<
;
;
          material (metal shavings and fasteners) was found in both exterior            l
panels and in the back board area in the switch house.
          panels and in the back board area in the switch house. The                     '
The
;         fasteners were removed on the spot. The effectiveness of rain                 ,
'
:          gutters on the switch house was minimal in deflecting water away-             t
;
i         from the structure, due to advanced corrosion.                                 l
fasteners were removed on the spot. The effectiveness of rain
                                                                                          l
,
          There was a number of areas where the licensee's repetitive
gutters on the switch house was minimal in deflecting water away-
          maintenance program for switchyard equipment was not consistent               !
t
          with the equipment manufacturer's recommendations. The licensee
:
i
from the structure, due to advanced corrosion.
l
l
There was a number of areas where the licensee's repetitive
maintenance program for switchyard equipment was not consistent
!
with the equipment manufacturer's recommendations. The licensee
;
'
'
                                                                                          ;
;
;          was unable to 3rovide documented justifications for the                       !
was unable to 3rovide documented justifications for the
          differences,   iowever, the licensee was able to provide anecdotal           .
!
          information, remembered by Transmission Maintenance Center
differences,
          personnel, that supported the differences.                                     l
iowever, the licensee was able to provide anecdotal
.
information, remembered by Transmission Maintenance Center
personnel, that supported the differences.
l
3
3
                                                                      Enclosure 2
Enclosure 2
;
;
*
*
.
_


    _, . _ .         _     _.     .
_, . _ .
                                        . ____ _ _ _ _ _ . _ . . _                           _ _ _ . _ ..
_
  .         .
_.
    ,
.
                                                                            11
. ____ _ _ _ _ _ . _ . . _
                                                                                                            <
_ _ _ . _
                      Transmission Maintenance Center records reflected that there were                   ,
..
                      19 repetitive maintenance tasks that were overdue, the oldest of
.
                      which had a due date of July 23, 1992. The overdue activities                       ;
.
                      were various 3reventative diagnos11c tests of air blast breakers.                     *
,
                      Transmission iaintenance Center records were such that timeliness                   .
11
                      of completed maintenance tasks could not be determined.
<
                                                                                                            !
Transmission Maintenance Center records reflected that there were
                c.   Conclusions
,
                                                                                                            '
19 repetitive maintenance tasks that were overdue, the oldest of
                      As demonstrated by good performance, the level of 3reventive
which had a due date of July 23, 1992.
                      maintenance for the Reactor Protection System and Reactor
The overdue activities
                      Recirculation System Motor Generators (MG) was a?propriate for the                   4
;
                      circumstances. Some housekeeping discrepancies were noted. The                       ,
were various 3reventative diagnos11c tests of air blast breakers.
                      lack of records that support differences from equipment                             I
*
                      manufacturer's areventive maintenance recommendations, and
Transmission iaintenance Center records were such that timeliness
                      dependance on t1e collective memory of personnel was not a good
.
                      practice.
of completed maintenance tasks could not be determined.
                      Due tc the switchyard housekee)ing and material condition
!
                      discrepancies identified and tie number and age of the predictive
c.
                      maintenance backlogged items, switchyard maintenance will be the
Conclusions
                      subject of a future NRC inspection. This matter will be
'
                      identified as Inspector Followup Item 50-321, 366/96-15-04:                           ;
As demonstrated by good performance, the level of 3reventive
                      Switchyard Maintenance and Material Condition.
maintenance for the Reactor Protection System and Reactor
                                                                                                            '
Recirculation System Motor Generators (MG) was a?propriate for the
                M2     Maintenance end Material Condition of Facilities and Equipment
4
!             'M2.1   Hydroaen Recombiner Unit 2
circumstances.
.                a.   Insoection Scooe (92902)
Some housekeeping discrepancies were noted. The
!                     On November 21. 1996, the ins)ectors observed that an 18-month
,
lack of records that support differences from equipment
I
manufacturer's areventive maintenance recommendations, and
dependance on t1e collective memory of personnel was not a good
practice.
Due tc the switchyard housekee)ing and material condition
discrepancies identified and tie number and age of the predictive
maintenance backlogged items, switchyard maintenance will be the
subject of a future NRC inspection. This matter will be
identified as Inspector Followup Item 50-321, 366/96-15-04:
;
Switchyard Maintenance and Material Condition.
'
M2
Maintenance end Material Condition of Facilities and Equipment
!
'M2.1
Hydroaen Recombiner Unit 2
a.
Insoection Scooe (92902)
.
!
On November 21. 1996, the ins)ectors observed that an 18-month
surveillance for the Unit 2A )rywell Hydrogen Recombiner System
-
-
                      surveillance for the Unit 2A )rywell Hydrogen Recombiner System
(HRS) could not be performed to due problems with inlet valve.
                      (HRS) could not be performed to due problems with inlet valve.
2T49-F003A. The controller for the valve was not operating
                      2T49-F003A. The controller for the valve was not operating
3roperly. The inspectors reviewed past performance and work
*
*
                        3roperly. The inspectors reviewed past performance and work
listory for the system. The system had been declared inoperable
                        listory for the system. The system had been declared inoperable
so that corrective maintenance could be completed.
                      so that corrective maintenance could be completed.                                     ;
i
                                                                                                              i
'
'
                b.   Observations and Findinas
b.
                      The inspectors reviewed documentation dated from November 20                         ,
Observations and Findinas
                      to 24, concerning the HRS and observed the following:
The inspectors reviewed documentation dated from November 20
1                     -       On November 20. the HRS 2A, Panel 2T49-P600A was removed from                 i
,
                              service for testing of motor operated valves (MOVs) and the                   i
to 24, concerning the HRS and observed the following:
                              replacement of MOV electrical overloads                                       !
1
                                                                                            Enclosure 2
-
                                                                    , , - ,   .-.y ., ,. _ ,, -
On November 20. the HRS 2A, Panel 2T49-P600A was removed from
i
service for testing of motor operated valves (MOVs) and the
i
replacement of MOV electrical overloads
Enclosure 2
, , - ,
.-.y
.,
,.
,,
-


    .
.
                                                      m u,       .a__._..uua-.m   .__..___,.2 -
m
                                                                                                            w.,
u,
                                                                                                                  I
.a__._..uua-.m
.    o                                                                                                           ;
.__..___,.2
  '                                                                                                               I
w.,
                                                                                                                  l
-
                                      12                                                                         :
I
        -  On November 21, the surveillance for the HRS valve operability                                       l
o
            was satisfactorily completed and the recombiner functional test                                     ]
;
            was started at 3:30 a.m.                                                                             !
.
                                                                                                                  !
'
        -
I
            On November 21. at 5:20 p.m., a functional test was                                                   l
l
              unsatisfactory due to a controller memory loss for inlet                                             '
12
            MOV 2T41-F003A. The loss of memory was due to a loss of power.                                       l
:
            The controller loses power when the breaker for the MOV is                                           <
On November 21, the surveillance for the HRS valve operability
              racked out.
l
        -
-
            On November 22 problems continued with valve 2T41-F003A. The                                         I
was satisfactorily completed and the recombiner functional test
              valve cycled partially open and closed and technicians were                                         !
]
            concerned that the motor on the valve would overheat, causing                                         ,
was started at 3:30 a.m.
            damage. The gain on the controller was adjusted with no affect
-
            and engineering personnel continued their investigation.                                             ;
On November 21. at 5:20 p.m., a functional test was
                                                                                                                  :
unsatisfactory due to a controller memory loss for inlet
        Licensee documentation revealed the problem was corrected and the
'
        2A HRS was returned to service at 11:45 p.m. on November 24.
MOV 2T41-F003A. The loss of memory was due to a loss of power.
        The inspectors identified from reviews and discussions with                                               f
The controller loses power when the breaker for the MOV is
        licensee personnel the following: the batteries located in the                                             ;
<
        flow controllers have a service life of five years, and a shelf
racked out.
                                                                                                                  '
-
        life of about three to four years, according to vendor                                                     !
On November 22 problems continued with valve 2T41-F003A. The
        information: the batteries had not been changed since Unit 2 was
valve cycled partially open and closed and technicians were
        licensed in 1978: and the batteries were installed in order to
concerned that the motor on the valve would overheat, causing
        protect the controllers from a loss of programming during a loss                                         ,
damage. The gain on the controller was adjusted with no affect
        of power.                                                                                                 l
and engineering personnel continued their investigation.
        The inspectors also identified that no procedure discussed the
;
        batteries, required that they be functionally tested, nor that
:
        they be changed in accordance with vendor recommendations.                       EDG
Licensee documentation revealed the problem was corrected and the
        3ersonnel responsible for the system failed to ensure that the                                           l
2A HRS was returned to service at 11:45 p.m. on November 24.
        3attery replacement was specified in plant procedures.                                                   :
The inspectors identified from reviews and discussions with
        The inspectors were later informed that, following maintenance
f
        activities on the valve a controller " dead band" was required to                                         ,
licensee personnel the following:
        be established for proper operation of the valve and valve
the batteries located in the
        controller. This requirement was also not identified in any                                               ,
;
        procedure, post maintenance testing, or calibration activity.                                             l
'
                                                                                                                  t
flow controllers have a service life of five years, and a shelf
        When the maintenance activities on the valve were completed. I&C                                         l
life of about three to four years, according to vendor
        completed the required calibrations and the old battery was                                               >
information: the batteries had not been changed since Unit 2 was
        tested. It satisfactorily performed. Since the licensee did not                                           !
licensed in 1978: and the batteries were installed in order to
        have a spare battery, the old one was left in place. The licensee                                         i
protect the controllers from a loss of programming during a loss
        initiated procurement activities to purchase a new battery.                                             .
,
        The inspectors verified that procedures were revised to identifv                           ~
of power.
                                                                                                                I
The inspectors also identified that no procedure discussed the
        establishing the require " dead band" following maintenance or                                           i
batteries, required that they be functionally tested, nor that
        calibration activities. The inspectors verified that procedures                                         ;
they be changed in accordance with vendor recommendations.
                                                                                  Enclosure 2
EDG
                                                                                                                !
3ersonnel responsible for the system failed to ensure that the
                                                                                                                .
l
                                                                                                                i
3attery replacement was specified in plant procedures.
                                                    .     -_ . _ . -.                             - _ - .
:
The inspectors were later informed that, following maintenance
activities on the valve a controller " dead band" was required to
,
be established for proper operation of the valve and valve
controller.
This requirement was also not identified in any
,
procedure, post maintenance testing, or calibration activity.
l
t
When the maintenance activities on the valve were completed. I&C
l
completed the required calibrations and the old battery was
>
tested.
It satisfactorily performed.
Since the licensee did not
!
have a spare battery, the old one was left in place.
The licensee
i
initiated procurement activities to purchase a new battery.
.
The inspectors verified that procedures were revised to identifv
I
~
establishing the require " dead band" following maintenance or
i
calibration activities. The inspectors verified that procedures
;
Enclosure 2
!
.
i
.
-
.
. -.
-
- .


,. ..
,.
..
i
i
,,
,,
                                        13
13
          were scheduled to be revised to include replacing the battery
were scheduled to be revised to include replacing the battery
          within the required vendor recommended frequency.
within the required vendor recommended frequency.
      c. Conclusions
c.
          The inspectors concluded from reviews and discussion with licensee
Conclusions
          personnel that the Unit 2 Drywell HRS flow controller batteries
The inspectors concluded from reviews and discussion with licensee
          exceeded the vendor recommended service life. Procedures were
personnel that the Unit 2 Drywell HRS flow controller batteries
            inadequate in that battery replacement was not identified.
exceeded the vendor recommended service life.
          Additionally, the procedures were inadequate for establishing the
Procedures were
            required valve controller " dead band" following certain
inadequate in that battery replacement was not identified.
          maintenance activities. This violation constitutes a violation of
Additionally, the procedures were inadequate for establishing the
          minor safety significance and is being identified as
required valve controller " dead band" following certain
          NCV 50-366/96-15-01: Inadequate Procedures for Replacement of the
maintenance activities. This violation constitutes a violation of
          Unit 2 Drywell Hydrogen Recombiner Flow Controller Batteries and
minor safety significance and is being identified as
          Establishing the Required Controller " Dead Band" Following Certain
NCV 50-366/96-15-01:
          Maintenance Activities, consistent with Section IV of the NRC
Inadequate Procedures for Replacement of the
          Enforcement Policy.
Unit 2 Drywell Hydrogen Recombiner Flow Controller Batteries and
      M3   Maintenance Procedures and Documentation
Establishing the Required Controller " Dead Band" Following Certain
      M3.1 Surveillance Observations
Maintenance Activities, consistent with Section IV of the NRC
                                                                                l
Enforcement Policy.
      a.   Insoection Scooe (61726)
M3
          The inspectors observed all or portions of the following Unit 1
Maintenance Procedures and Documentation
          and Unit 2 surveillance activities:
M3.1 Surveillance Observations
            - 345V-E41-002-15: HPCI Pump Operability.. Revision (Rev.) 19
a.
            - 34SV-R43-001-1S: DG 1A Monthly Test, Rev. 17. ED 1
Insoection Scooe (61726)
            - 34SV-E41-002-2S: HPCI Pump Operability. Rev. 23
The inspectors observed all or portions of the following Unit 1
            - 34SV-E51-002-1S: RCIC Pump Operability. Rev. 17
and Unit 2 surveillance activities:
            - 34SV-E51-002-2S: RCIC Pump Operability. Rev. 16
- 345V-E41-002-15: HPCI Pump Operability.. Revision (Rev.) 19
      b. Observations and Findinas
- 34SV-R43-001-1S: DG 1A Monthly Test, Rev. 17. ED 1
          On December 26, the inspectors attended the pre-job briefing in
- 34SV-E41-002-2S: HPCI Pump Operability. Rev. 23
          preparation for the Unit 1 High Pressure Core Injection (HPCI)
- 34SV-E51-002-1S:
          surveillar,ce activities and observed operator actions during
RCIC Pump Operability. Rev. 17
          portions of the surveillance. The test was also >erformed to meet
- 34SV-E51-002-2S:
          the Inservice Testing (IST) requirements for the iPCI system. The
RCIC Pump Operability. Rev. 16
            inspectors observed that a member of engineering su) port,
b.
          maintenance, health physics (HP), o)erations and t1e system
Observations and Findinas
          engineer were present at the pre-jo) briefing. The Assistant
On December 26, the inspectors attended the pre-job briefing in
          General Manager - Plant Support (AGM-PS) was present for the
preparation for the Unit 1 High Pressure Core Injection (HPCI)
          majority of the briefing.
surveillar,ce activities and observed operator actions during
          During the briefing, operations personnel requested that HP ensure   j
portions of the surveillance.
          that no personnel were in the torus area. This was for personnel     l
The test was also >erformed to meet
          protection, based upon previous industry operating event history
the Inservice Testing (IST) requirements for the iPCI system.
                                                                    Enclosure 2
The
                                                                                l
inspectors observed that a member of engineering su) port,
                                                                                l
maintenance, health physics (HP), o)erations and t1e system
                                                                                J
engineer were present at the pre-jo) briefing.
The Assistant
General Manager - Plant Support (AGM-PS) was present for the
majority of the briefing.
During the briefing, operations personnel requested that HP ensure
j
that no personnel were in the torus area.
This was for personnel
protection, based upon previous industry operating event history
Enclosure 2
J


,-
,-
l
l
    *
*
  .
.
I
I
                                        14
14
i
i
          for failure of small turbine exhaust diaphragms. HP personnel
for failure of small turbine exhaust diaphragms.
          ensured that no personnel were in the area and posted it.
HP personnel
          The inspectors observed that hydrogen injection was lowered to
ensured that no personnel were in the area and posted it.
          about 8 standard cubic feed per minute (SCFM) and that the
The inspectors observed that hydrogen injection was lowered to
          applicable technical requirements manual (TRM) action statement
about 8 standard cubic feed per minute (SCFM) and that the
          for the main steam line radiation monitors being set
applicable technical requirements manual (TRM) action statement
for the main steam line radiation monitors being set
non-conservatively was entered.
3
3
          non-conservatively was entered.
The inspectors observed that a HP technical was present locally
          The inspectors observed that a HP technical was present locally
and had identified the HPCI room as a High radiation area. A
          and had identified the HPCI room as a High radiation area. A
minimal number of personnel entered the HPCI room during
          minimal number of personnel entered the HPCI room during
operation, consistent with As low As Reasonably Achievable (ALARA)
          operation, consistent with As low As Reasonably Achievable (ALARA)
considerations. Maintenance and other personnel were on standby
          considerations. Maintenance and other personnel were on standby
at a designated low dose area.
          at a designated low dose area.
The inspectors observed that operator actions in the control room
          The inspectors observed that operator actions in the control room
were adequate. Appropriate attention to detail, procedural usage,
          were adequate. Appropriate attention to detail, procedural usage,
and supervisory oversight were demonstrated. Communications were
          and supervisory oversight were demonstrated. Communications were
not all 3-part, but did not present any observable problems during
          not all 3-part, but did not present any observable problems during
The i'spectors discussed operator
          the surveillance. The i'spectors
the surveillance.
                                    n       discussed operator
n
          communications during the surveillance and general communications     :
communications during the surveillance and general communications
          with operations * management. Operations * management stated that a   j
:
          renewed emphasis had been placed on communications and that some
with operations * management. Operations * management stated that a
          crews demonstrated better communications than others.
j
          The inspectors toured the EDG building and observed the 1A EDG
renewed emphasis had been placed on communications and that some
          during the surveillance run. The inspectors identified a small
crews demonstrated better communications than others.
          oil leak on the governor that had not been previously identified.
The inspectors toured the EDG building and observed the 1A EDG
          The leak was brought to the attention of operators stationed at
during the surveillance run. The inspectors identified a small
          the EDG who contacted maintenance personnel, who repaired the
oil leak on the governor that had not been previously identified.
          leak
The leak was brought to the attention of operators stationed at
      c. Conclusions
the EDG who contacted maintenance personnel, who repaired the
          The Unit 1 HPCI and EDG systems performed as required and met the
leak
          ap)licable TS criteria. However, the HPCI pump outboard bearing
c.
          vi) ration increased to the alert range. requiring that the
Conclusions
          surveillance test frequency for HPCI pump be doubled. The
The Unit 1 HPCI and EDG systems performed as required and met the
          performance of the operators and crews conducting the
ap)licable TS criteria.
          surveillances was generally professional and competent. The
However, the HPCI pump outboard bearing
          inspectors had observed some improvements in communications in the
vi) ration increased to the alert range. requiring that the
          recent past but observed that operations * standards were not met
surveillance test frequency for HPCI pump be doubled.
          by all crews.   No other deficiencies were identified.
The
                                                                    Enclosure 2
performance of the operators and crews conducting the
surveillances was generally professional and competent.
The
inspectors had observed some improvements in communications in the
recent past but observed that operations * standards were not met
by all crews.
No other deficiencies were identified.
Enclosure 2


                                                                          _   __
,
    ,
_
      *
__
(
*
.
.
  -                                                                                 (
-
                                                                                    ,
,
                                                                                    !
!
                                            15                                     i
15
                                                                                    t
i
        H3.2 Review of Maintenance Activities to Electrically Backseat Valves.     !
t
        a.   Insoection Scooe (62703)                                             ;
H3.2 Review of Maintenance Activities to Electrically Backseat Valves.
                                                                                    ;
!
              The inspectors reviewed maintenance activities and documentation       i
a.
              for electrically backseating two Primary Containment Isolation       '
Insoection Scooe (62703)
              valves. The licensee electrically backseated the valves in an         i
;
              attempt to identify and reduce the unidentified drywell leakage-       f
;
              for Unit 1.   Reactor Water Cleanup (RWCU) Inboard Isolation         j
The inspectors reviewed maintenance activities and documentation
              valve 1G31-F001, and RCIC Inboard Isolation valve 1E51-F007. were     !
i
              electrically backseated on November 14 and December 27. 1996.         i
for electrically backseating two Primary Containment Isolation
                                                                                    '
'
              respectfully. The inspectors reviewed the corporate engineering
valves. The licensee electrically backseated the valves in an
              evaluation (section E3.1 of this report) to ensure that all
i
              a>plicable actions were completed. Additional inspector
attempt to identify and reduce the unidentified drywell leakage-
              o)servations are discussed in section E3.1 of this report.
f
                                                                                      '
for Unit 1.
        b.   Observations and Findinas.
Reactor Water Cleanup (RWCU) Inboard Isolation
            The inspectors reviewed procedure 51GM-MNT-034-05:     MOV Electrical f
j
              Backseating With Instantaneous Circuit Breaker Trip Protection,         j
valve 1G31-F001, and RCIC Inboard Isolation valve 1E51-F007. were
              Rev. 2. The following are deficiencies that were identified by the
!
                                                                                      '
electrically backseated on November 14 and December 27. 1996.
              inspectors:
i
                                                                                      '
'
              -
respectfully. The inspectors reviewed the corporate engineering
                  The Evaluation section of the corporate engineering evaluation
evaluation (section E3.1 of this report) to ensure that all
                  stated that procedure 51GM-MNT-034-05, limits the motor current
a>plicable actions were completed. Additional inspector
                  (of the valve being backseated) to twice the rated current.
o)servations are discussed in section E3.1 of this report.
                  However, step 7.6 of the procedure states, in part, to " adjust
b.
                  breaker 2 on the backseat apparatus to 2 times rated amps
Observations and Findinas.
                  (+/- 50%)." This would allow a maximum of three times rated
'
                  motor current, not twice the motor current, as s)ecified in the
The inspectors reviewed procedure 51GM-MNT-034-05:
                  engineering evaluation. Engineering concluded tlat this
MOV Electrical
                  difference was not a safety concern for the valve since the
f
                  engineering evaluation was more concerned with locked rotor
Backseating With Instantaneous Circuit Breaker Trip Protection,
                  current.
j
              -
Rev. 2. The following are deficiencies that were identified by the
                  Special requirements. Step 4.3.2 of the backseating procedure
'
                  and the engineering evaluation, states, in part, that prior to
inspectors:
                  performing backseating, the Shift Supervisor on duty will
'
                  review the engineering evaluation for the impact on stroke time
-
                  requirements and will indicate the results cf Ms review in the
The Evaluation section of the corporate engineering evaluation
                  work performed section of the MW0.
stated that procedure 51GM-MNT-034-05, limits the motor current
                  This documentation was not completed for either of the two
(of the valve being backseated) to twice the rated current.
                  valves that were backseated. The inspectors discussed this
However, step 7.6 of the procedure states, in part, to " adjust
                  deficiency with maintenance and operations personnel. The
breaker 2 on the backseat apparatus to 2 times rated amps
                  operations supervisor on shift during one of the backseating
(+/- 50%)." This would allow a maximum of three times rated
                  activities stated that he did not review the maintenance
motor current, not twice the motor current, as s)ecified in the
                  procedure and was not aware of the documentation requirement.
engineering evaluation.
                  The inspectors discussed maintenance activities with respect to
Engineering concluded tlat this
                                                                        Enclosure 2
difference was not a safety concern for the valve since the
engineering evaluation was more concerned with locked rotor
current.
-
Special requirements. Step 4.3.2 of the backseating procedure
and the engineering evaluation, states, in part, that prior to
performing backseating, the Shift Supervisor on duty will
review the engineering evaluation for the impact on stroke time
requirements and will indicate the results cf Ms review in the
work performed section of the MW0.
This documentation was not completed for either of the two
valves that were backseated. The inspectors discussed this
deficiency with maintenance and operations personnel.
The
operations supervisor on shift during one of the backseating
activities stated that he did not review the maintenance
procedure and was not aware of the documentation requirement.
The inspectors discussed maintenance activities with respect to
Enclosure 2


    _
_
.
.
.
16
reviewing procedures prior to their use and how maintenance
communicated specific requirements to operations personnel. The
inspectors were informed that if a maintenance procedure
contained specific requirements for operations personnel,
maintenance personnel were required to bring the requirement to
the attention of operations.
,
i
The inspectors reviewed procedure 10AC-MGR-019-05:
Procedure
l
Use and Adherence Rev. O, and observed that step 4.3.4,
!
stated, in part, that all plant personnel were responsible ~for
.
reviewing and understanding procedures prior to using them.
The inspectors concluded that in at least one example discussed
above, maintenance personnel responsible for the valve
backseating procedure did not bring the specific documentation
requirement to the attention of operations' supervision. The
,
inspectors noted that after bringing the deficiency to the
;
attention of the maintenance personnel..the documentation was
:
later completed.
:
i
During the discussion with maintenance personnel concerning
!
procedure use, the inspectors were informed that some sections
:
of maintenance procedures may be considered continuous use,
-
some sections may be considered reference use, and other parts
;
may be considered information use. The inspectors discussed
;
different procedure usage with at least five different
i
maintenance personnel and discovered that no clear
understanding of procedure usage was evident. The inspectors
.
.
      .
reviewed Procedure 10AC-MGR-019-0S. Rev. O. and discussed
  .
!
                                      16
procedure usage with maintenance management. The inspectors
            reviewing procedures prior to their use and how maintenance
i
            communicated specific requirements to operations personnel. The
were informed that improvement in procedure usage continued to
            inspectors were informed that if a maintenance procedure
be a challenge and management's expectations were not being
            contained specific requirements for operations personnel,
!
            maintenance personnel were required to bring the requirement to
met.
            the attention of operations.                                      ,
,
                                                                              i
!
            The inspectors reviewed procedure 10AC-MGR-019-05:    Procedure    l
It was not clear to the inspectors how some personnel's
            Use and Adherence Rev. O, and observed that step 4.3.4,            !
;
            stated, in part, that all plant personnel were responsible ~for
misunderstanding of procedure usage would ensure effective and
            reviewing and understanding procedures prior to using them.        .
i
            The inspectors concluded that in at least one example discussed
consistent implementation of the procedures.
            above, maintenance personnel responsible for the valve
Procedure usage
            backseating procedure did not bring the specific documentation
j
            requirement to the attention of operations' supervision. The        ,
appeared to be very subjective on the part of the user and
            inspectors noted that after bringing the deficiency to the          ;
!
            attention of the maintenance personnel..the documentation was      :
would not necessarily ensure that management's expectations for
            later completed.                                                  :
i
                                                                                i
procedure usage were consistently met.
            During the discussion with maintenance personnel concerning        !
The inspectors
            procedure use, the inspectors were informed that some sections      :
'
            of maintenance procedures may be considered continuous use,
concluded that maintenance personnel's understanding of
        -
different procedure usage and implementation demonstrated a
            some sections may be considered reference use, and other parts      ;
,
            may be considered information use. The inspectors discussed        ;
weakness.
            different procedure usage with at least five different              i
-
            maintenance personnel and discovered that no clear
-
            understanding of procedure usage was evident. The inspectors        .
Procedure step 4.3.4 stated, in part. that the engineering
            reviewed Procedure 10AC-MGR-019-0S. Rev. O. and discussed         !
,
            procedure usage with maintenance management. The inspectors       i
evaluation must be attached to Attachment 1 of the procedure
            were informed that improvement in procedure usage continued to
i
            be a challenge and management's expectations were not being       !
and filed in Document Control with a copy attached to the MWD.
            met.                                                               ,
:
                                                                              !
The inspectors observed that during the review of the MWO work
            It was not clear to the inspectors how some personnel's           ;
[
            misunderstanding of procedure usage would ensure effective and     i
package for the backseating completed on November 14 the
            consistent implementation of the procedures. Procedure usage     j
Enclosure 2
            appeared to be very subjective on the part of the user and         !
!
            would not necessarily ensure that management's expectations for   i
I
                                                                              '
f
            procedure usage were consistently met. The inspectors
:
            concluded that maintenance personnel's understanding of
!
            different procedure usage and implementation demonstrated a       ,
L
                                                                              -
            weakness.
          -
            Procedure step 4.3.4 stated, in part. that the engineering         ,
            evaluation must be attached to Attachment 1 of the procedure     i
            and filed in Document Control with a copy attached to the MWD.   :
            The inspectors observed that during the review of the MWO work   [
            package for the backseating completed on November 14 the
                                                                  Enclosure 2
                                                                              !
                                                                              I
                                                                              f
                                                                              :
                                                                              !
                                                                              L


      .- .   --- --               -.   -         .     - - - -.   . - - ~_.-.           _   _ - -
.- .
                                                                                                      .
--- --
                                                                                                      !
-.
            $                                                                                         i
-
    .
.
                                                                                                      ;
- - - -.
                                                                                                      i
. - - ~_.-.
                                                        17
_
.                          engineering evaluation was not part of the MWO work package and           )
_ - -
                            was not attached to Attachment 1. The inspectors noted that
.
!
i
$
.
i
17
engineering evaluation was not part of the MWO work package and
)
.
#
#
                                                                                                      !
was not attached to Attachment 1.
;                         the MWO work package was being maintained open until after
The inspectors noted that
;                           outage work. After bringing this deficiency to the attention
!
j                           of maintenance personnel. the engineering evaluation was                   ;
;
:                           included as-part of the MWO package and properly attached to               i
the MWO work package was being maintained open until after
!                           the procedure.                                                             j
;
;                                                                                                     ;
outage work. After bringing this deficiency to the attention
.
j
                          -
of maintenance personnel. the engineering evaluation was
                            v._adure step 4.3.5 stated. in part, that a MWO must be                   i
;
                            initiated for internal inspection on the valve to be                       i
:
j                           backseated.                                                               l
included as-part of the MWO package and properly attached to
i
!
the procedure.
j
;
;
.
v._adure step 4.3.5 stated. in part, that a MWO must be
i
-
initiated for internal inspection on the valve to be
i
j
backseated.
The inspectors observed that the engineering evaluation did not
l
-
specify that an internal inspection of the valve be completed.
i
.
i
However, the evaluation identified that the procedure required
an internal inspection of the valve that was backseated.
The
,
inspectors observed that a MWO was not initiated for an
internal inspection of the valve backseated on December 27.
During a discussion with the system engineer he indicated that
i
-
-
                            The inspectors observed that the engineering evaluation did not            l
.                          specify that an internal inspection of the valve be completed.            i
i                          However, the evaluation identified that the procedure required
                            an internal inspection of the valve that was backseated. The              ,
                            inspectors observed that a MWO was not initiated for an                    !
                            internal inspection of the valve backseated on December 27.
-                          During a discussion with the system engineer he indicated that              i
                                                                                                        '
!                          an internal valve inspection would be completed provided other
                            inspections of the valve and or actuator indicated that an
j                          internal inspection was warranted.
i                          For the valve backseated on November 14. the MWO identified                  l
l                          that an internal valve ins)ection be performed but referenced
'
'
                            an incorrect procedure. T1e procedure referenced and
!
!                           documented on the MWO did not exist. This deficiency was
an internal valve inspection would be completed provided other
inspections of the valve and or actuator indicated that an
j
internal inspection was warranted.
i
For the valve backseated on November 14. the MWO identified
l
that an internal valve ins)ection be performed but referenced
an incorrect procedure.
T1e procedure referenced and
'
!
documented on the MWO did not exist.
This deficiency was
maintenance personnel. pectors identified the problem to
corrected after the ins
'
'
                            corrected after the ins
4
4
                            maintenance personnel. pectors identified the problem to
l
l                        -
-
                            The engineering evaluation recommended that o)erations
The engineering evaluation recommended that o)erations
:                           implement administrative controls to ensure tlat the backseated
:
l                           valves would be removed from backseat prior to a 100 degree
implement administrative controls to ensure tlat the backseated
                            Fahrenheit ( F) cooldown of the reactor. Operations placec
l
                            caution tags on the valves to meet this recommendation.
valves would be removed from backseat prior to a 100 degree
Fahrenheit ( F) cooldown of the reactor.
Operations placec
caution tags on the valves to meet this recommendation.
The inspectors observed the caution tags placed on the
i
i
                            The inspectors observed the caution tags placed on the
backseated valves and noted that the caution tags stated that
                            backseated valves and noted that the caution tags stated that
:
:                           the valves were electrically backseated. The caution tag book
the valves were electrically backseated.
The caution tag book
did not contain any additional information.
The inspectors
>
>
                            did not contain any additional information. The inspectors
                                                                                  .
                            reviewed procedure 34G0-0PS-013-2S:      Normal Plant Shutdown.
                            Rev. 21. and observed that step 7.3.26 stated, in part, that
!                            3rior to cooldown greater than 100 F. remove all MOVs that have
                            3een electrically or manually backseated from their backseat.
                            The procedure did not provide additional instructions for the
                            activity.
.
.
                            The ins)ectors discussed a concern with operations' management
reviewed procedure 34G0-0PS-013-2S:
Normal Plant Shutdown.
Rev. 21. and observed that step 7.3.26 stated, in part, that
!
3rior to cooldown greater than 100 F. remove all MOVs that have
3een electrically or manually backseated from their backseat.
The procedure did not provide additional instructions for the
activity.
.
The ins)ectors discussed a concern with operations' management
as to w1 ether the operators had sufficient guidance for
,
removing valves from their backseated condition during all
,
,
                            as to w1 ether the operators had sufficient guidance for
.
Enclosure 2
i
I
i
i
'
_
,
,
                            removing valves from their backseated condition during all
_ _ _ .
.                                                                                    Enclosure 2        i
_
                                                                                                        I
, _ . . _
  i
-
  '
_
                                                                                                        i
.
                                                                                                        !
    _    ,    _ _ _ . _       , _ . . _         -   _
                                                                  ._


  ~
~
    ,
,
.,
.,
                                          18
18
                  plant conditions. The normal method of removing a valve from
plant conditions. The normal method of removing a valve from
                  its backseat was to close the valve using the control room
its backseat was to close the valve using the control room
                  handswitch. The inspectors concern was that if operators used
handswitch. The inspectors concern was that if operators used
                  this method of removing valves from their backseat. RCIC and
this method of removing valves from their backseat. RCIC and
                  RWCU system (and other systems with backseated valves) would be
RWCU system (and other systems with backseated valves) would be
                  isolated when they may be needed for continued safe unit
isolated when they may be needed for continued safe unit
                  shutdown.   As a result of this discussion operations'
shutdown.
                management provided additional instructions for the beginning
As a result of this discussion operations'
                  of shift training (BOST) for each operating crew informing
management provided additional instructions for the beginning
                  them of expectations and priorities during plant transient
of shift training (BOST) for each operating crew informing
                  conditions. The inspectors did not identify similar
them of expectations and priorities during plant transient
                  instructions in the unit's scram proced r e.
conditions. The inspectors did not identify similar
        c.   Conclusions
instructions in the unit's scram proced r e.
            The inspectors concluded that failure to follow procedures
c.
            51GM-MNT-034-OS and 10 AC-MGR-019-0S by maintenance personnel to
Conclusions
            ensure that steps were completed was a violation. This was
The inspectors concluded that failure to follow procedures
            identified as Violation 50-321/96-15-02: Maintenance Personnel
51GM-MNT-034-OS and 10 AC-MGR-019-0S by maintenance personnel to
            Failure To Follow Procedure During Valve Backseating Activities.
ensure that steps were completed was a violation.
            The inspectors concluded that maintenance personnel's lack of
This was
            understandina of the different types of procedure usage
identified as Violation 50-321/96-15-02: Maintenance Personnel
            requirements and implementation demonstrated a weakness.
Failure To Follow Procedure During Valve Backseating Activities.
            The inspectors concluded that the maintenance procedure for
The inspectors concluded that maintenance personnel's lack of
            electrically backseating valves did not fully implement the
understandina of the different types of procedure usage
            requirements of the engineering evaluation. The inspectors
requirements and implementation demonstrated a weakness.
            concluded that this deficiency did not result in a safety
The inspectors concluded that the maintenance procedure for
            significant concern for the backseated valves.
electrically backseating valves did not fully implement the
      M3.3 Unit 1 RCIC and Unit 2 HPCI Soeed Control Chances
requirements of the engineering evaluation.
        a.   Insoection Scooe (92902)
The inspectors
            The ins)ectors observed upward drifts in the Unit 1 RCIC and
concluded that this deficiency did not result in a safety
            Unit 2 iPCI turbine speed controls during the 3erformance of
significant concern for the backseated valves.
            surveillance tests. The drifting occurred wit 1out operator
M3.3 Unit 1 RCIC and Unit 2 HPCI Soeed Control Chances
            actions. The inspectors reviewed and discussed the results of the
a.
            Unit 2 RCIC test performed on January 9 with operations and
Insoection Scooe (92902)
            engineering personnel. The inspectors also observed a
The ins)ectors observed upward drifts in the Unit 1 RCIC and
            post-maintenance test of the Unit 2 RCIC system on January 10 (See
Unit 2 iPCI turbine speed controls during the 3erformance of
            Section M1.3).
surveillance tests. The drifting occurred wit 1out operator
        b. Observations and Findinas
actions. The inspectors reviewed and discussed the results of the
            The inspectors observed, reviewed, and discussed the results of
Unit 2 RCIC test performed on January 9 with operations and
            the operability surveillance tests for the Unit 1 RCIC Pump and
engineering personnel.
            the Unit 2 HPCI Pump. The ins)ectors also observed maintenance
The inspectors also observed a
            activities for the repair of t1e Unit 2 RCIC pump. The inspectors
post-maintenance test of the Unit 2 RCIC system on January 10 (See
                                                                      Enclosure 2
Section M1.3).
b.
Observations and Findinas
The inspectors observed, reviewed, and discussed the results of
the operability surveillance tests for the Unit 1 RCIC Pump and
the Unit 2 HPCI Pump.
The ins)ectors also observed maintenance
activities for the repair of t1e Unit 2 RCIC pump.
The inspectors
Enclosure 2


                                                                          .m, -. _ -. . - ,...
.m,
  .
-.
      '
_
    ,
-. . - ,...
'
.
,
19
-
attended the operations pre-job and post-job briefings..
The
briefings were thorough and stressed effective communications,
procedure adherence. job assignments, responsibilities, and test
results.
The inspectors observed the following during the Unit 1 RCIC
turbine test:
-
The RCIC pump turbine was manually started and after one minute
into the test the turbine speed appeared to stabilize at about
4460 revolutions per minute (rpm), as required oy procedure
-
At approximately four minutes into the test the turbine speed
drifted up to 4500 rpm
-
The operator took control of the turbine and lowered the speed
to 4460 rpm and at eight minutes into the test the turbine
appeared to stabilize at that speed
-
At approximately 15 minutes into the test the turbine speed
started to drift up again
-
-
                                      19
The test was completed at approximately 25 minutes and the
        attended the operations pre-job and post-job briefings.. The
turbine speed had drifted up to 4490 rpm
        briefings were thorough and stressed effective communications,
The inspectors reviewed test results data which verified what the
        procedure adherence. job assignments, responsibilities, and test
ins)ectors had observed concerning the upward drift of the RCIC
        results.
tur)ine speed.
        The inspectors observed the following during the Unit 1 RCIC
During discussions with operators and engineers,
        turbine test:
the inspectors were informed that the Control Room (CR) turbine
        -
speed indication was 100 rpm lower than the actual turbine speed.
            The RCIC pump turbine was manually started and after one minute
The inspectors observed the following during the Unit 2 HPCI
              into the test the turbine speed appeared to stabilize at about
turbine test:
            4460 revolutions per minute (rpm), as required oy procedure
The HPCI turbine was started, came up to set speed, and
        -
-
            At approximately four minutes into the test the turbine speed
appeared to stabilize at 3865 rpm
            drifted up to 4500 rpm
-
        -
Shortly after the speed stabilized, a gradual upward drift
            The operator took control of the turbine and lowered the speed
began. At the end of the test, which lasted for 21 minutes,
            to 4460 rpm and at eight minutes into the test the turbine
the turbine appeared to be controlling at 3910 rpm
            appeared to stabilize at that speed
-
        -
The lowest rpm observed by the inspectors was 3862 and the
            At approximately 15 minutes into the test the turbine speed
highest was 3918 rpm
            started to drift up again
The inspectors found from the observations, discussions and
        -
reviews taat the upward drift of the Unit 1 RCIC turbine speed was
            The test was completed at approximately 25 minutes and the
not expected.
            turbine speed had drifted up to 4490 rpm
The turbine speed drift should not have occurred
        The inspectors reviewed test results data which verified what the
because of the design of the system. The system should have
        ins)ectors had observed concerning the upward drift of the RCIC
stabilized around 4460 rpm instead of having a constant upward
        tur)ine speed. During discussions with operators and engineers,
l
        the inspectors were informed that the Control Room (CR) turbine
Enclosure 2
        speed indication was 100 rpm lower than the actual turbine speed.
j
        The inspectors observed the following during the Unit 2 HPCI
i
        turbine test:
-
        -
. . --, -._-
            The HPCI turbine was started, came up to set speed, and
- -
            appeared to stabilize at 3865 rpm
        -
            Shortly after the speed stabilized, a gradual upward drift
            began. At the end of the test, which lasted for 21 minutes,
            the turbine appeared to be controlling at 3910 rpm
        -
            The lowest rpm observed by the inspectors was 3862 and the
            highest was 3918 rpm
        The inspectors found from the observations, discussions and
        reviews taat the upward drift of the Unit 1 RCIC turbine speed was
        not expected. The turbine speed drift should not have occurred
        because of the design of the system. The system should have
        stabilized around 4460 rpm instead of having a constant upward                         ;
                                                                                              l
                                                                                              l
                                                                  Enclosure 2                 j
                                                                                              l
                                                                                              l
                                                                                              i
                                                                                              l


-
-
    '
'
  .
.
                                        20
20
            drift.   The system engineer, stationed locally at the Unit 1 RCIC
drift.
            pump, assumed that the upward drift was due to operator action.
The system engineer, stationed locally at the Unit 1 RCIC
          The upward drift observed on the Unit 2 HPCI turbine continued
pump, assumed that the upward drift was due to operator action.
            throughout the test. The inspector discussed the observation of
The upward drift observed on the Unit 2 HPCI turbine continued
            the drift with operations personnel. Licensee personnel discussed
throughout the test. The inspector discussed the observation of
            several possibilities for the deficiencies which included out of
the drift with operations personnel.
          calibration electronics, a test valve gradually clogging up with
Licensee personnel discussed
          debris, or a mechanical malfunction of the test valve.                 !
several possibilities for the deficiencies which included out of
          Subsequent to the Unit 1 RCIC turbine test a Unit 2 RCIC turbine
calibration electronics, a test valve gradually clogging up with
          test was performed. During the test the operators observed             i
debris, or a mechanical malfunction of the test valve.
            significant changes in the speed of the Unit 2 RCIC turbine. The
!
            I&C technicians informed the operators that the turbine control       i
Subsequent to the Unit 1 RCIC turbine test a Unit 2 RCIC turbine
                                                                                  '
test was performed.
          valve was receiving full open signals followed by full closed
During the test the operators observed
          signals on a continuous basis. The turbine control valve appeared
i
          to go to the fully open position and immediately go to the fully
significant changes in the speed of the Unit 2 RCIC turbine. The
          closed position. This caused observed fluctuations in turbine
I&C technicians informed the operators that the turbine control
          speed of up to plus-or-minus 160 rpm. The operators declared the
i
          Unit 2 RCIC system inoperable.   The RCIC system engineer informed
'
          the ins)ectors that the Unit 2 RCIC system would operate in this
valve was receiving full open signals followed by full closed
          manner   )ut not for very long. The inspectors observed the
signals on a continuous basis.
          post-maintenance test of the Unit 2 RCIC and did not observe any
The turbine control valve appeared
          deficiencies.
to go to the fully open position and immediately go to the fully
      c. Conclusions
closed position.
          The inspectors concluded that the maximum drift observed on the
This caused observed fluctuations in turbine
          Unit 1 RCIC turbine was 40 rpm. The upward drift of the Unit 2
speed of up to plus-or-minus 160 rpm. The operators declared the
          HPCI turbine was about 45 rpm. The inspectors concluded that the
Unit 2 RCIC system inoperable.
          drifts could be an indication of pending failures. The erratic
The RCIC system engineer informed
          speed control of the Unit 2 RCIC was a significant problem. This
the ins)ectors that the Unit 2 RCIC system would operate in this
          was identified as IFI 50-321, 366/96-15-03:   Resolution of RCIC
manner )ut not for very long.
          and HPCI Turbine Speed Control Drift Units 1 and 2. respectively.
The inspectors observed the
      M4   Maintenance Staff Knowledge and Performance
post-maintenance test of the Unit 2 RCIC and did not observe any
      M4.1 Inadvertent Feedwater Heater Isolation.
deficiencies.
      a. Insoection Scooe (62707)                                             J
c.
          The inspectors conducted a review of maintenance work activities,
Conclusions
          reviewed documentation and discussed maintenance personnel
The inspectors concluded that the maximum drift observed on the
          performance with licensee personnel with respect to an inadvertent
Unit 1 RCIC turbine was 40 rpm.
          isolation of a Unit 2 feedwater heater,
The upward drift of the Unit 2
      b. Observations and Findinas
HPCI turbine was about 45 rpm. The inspectors concluded that the
          On January 5, during maintenance activities to replace a relay on
drifts could be an indication of pending failures.
          the 6th stage A heater steam trap bypass to the condenser. a fuse
The erratic
                                                                    Enclosure 2
speed control of the Unit 2 RCIC was a significant problem. This
was identified as IFI 50-321, 366/96-15-03:
Resolution of RCIC
and HPCI Turbine Speed Control Drift Units 1 and 2. respectively.
M4
Maintenance Staff Knowledge and Performance
M4.1
Inadvertent Feedwater Heater Isolation.
a.
Insoection Scooe (62707)
J
The inspectors conducted a review of maintenance work activities,
reviewed documentation and discussed maintenance personnel
performance with licensee personnel with respect to an inadvertent
isolation of a Unit 2 feedwater heater,
b.
Observations and Findinas
On January 5, during maintenance activities to replace a relay on
the 6th stage A heater steam trap bypass to the condenser. a fuse
Enclosure 2


        .
                .    .. . - . _ - _ .  .-. --              -- - _ ..- - -
    .
.
.
      .
.
  .
.
                                        21
.. . - .
          blew.   As a result, steam from the high pressure turbine to the
_ - _ .
          6th stage heaters was isolated, causing feedwater heater levels to
.-. --
          become erratic.
-- - _ ..- - -
          Operators observed that feedwater temperature decreased and
.
          entered the abnormal procedure for loss of feedwater temperature.
.
          Power was reduced to about 93.5% RTP. The blown fuse was
.
          replaced, heater levels were stabilized and power was later
21
          returned to 100% RTP. The relay, which remained in the energized
blew.
          state even though the relay fuse had blown, was not immediately
As a result, steam from the high pressure turbine to the
          replaced. The relay was replaced the following day after a work
6th stage heaters was isolated, causing feedwater heater levels to
          plan was completed by engineering and maintenance personnel. The
become erratic.
          inspectors noted that while similar relays had failed, sticking in
Operators observed that feedwater temperature decreased and
          the energized condition was an unusual case.
entered the abnormal procedure for loss of feedwater temperature.
          The inspectors reviewed procedure 34AB-N21-001-2S:               Loss of
Power was reduced to about 93.5% RTP. The blown fuse was
          Feedwater Heating. Revision 2. and observed that operators
replaced, heater levels were stabilized and power was later
          initiated the correct actions for the plant transient.
returned to 100% RTP.
          The inspectors discussed maintenance personnel's actions involved
The relay, which remained in the energized
          with the relay replacement with maintenance supervision. The
state even though the relay fuse had blown, was not immediately
          inspectors were informed that an I&C technician was in the process
replaced.
          of jumpering out the relay to be replaced had connected one end
The relay was replaced the following day after a work
          of the jumper to a hot lead, and was routing the jumper through
plan was completed by engineering and maintenance personnel. The
          the panel toward the other lead that was to be jumpered. The
inspectors noted that while similar relays had failed, sticking in
          jumper was inadvertently grounded blowing the fuse, and
the energized condition was an unusual case.
          initiating the transient.
The inspectors reviewed procedure 34AB-N21-001-2S:
          The inspectors discussed expectations for jumper usage with
Loss of
          maintenance management.     Management indicated that connecting a
Feedwater Heating. Revision 2. and observed that operators
          jumper to a hot lead and then routing it through a panel did not
initiated the correct actions for the plant transient.
          meet their expectations. The inspectors reviewed several
The inspectors discussed maintenance personnel's actions involved
          maintenance procedures and observed that general jumper usage and
with the relay replacement with maintenance supervision.
          expectations for jumper usage was lacking.
The
          In April and May 1995. the licensee conducted an extensive review
inspectors were informed that an I&C technician was in the process
          of jumper types, and jumper usage at the site. This review was
of jumpering out the relay to be replaced had connected one end
          conducted as a result of a reactor scram following operator
of the jumper to a hot lead, and was routing the jumper through
          deficiencies using jumpers. The inspectors observed that as a
the panel toward the other lead that was to be jumpered.
          result of this licensee review, several recommendations for jumper
The
          types and jumper usage, and written expectations were developed.
jumper was inadvertently grounded blowing the fuse, and
          Most departments held special training sessions for jumper usage
initiating the transient.
          and the proper types of jumpers to be used. Operations issued a
The inspectors discussed expectations for jumper usage with
          special procedure detailing operations management's expectations
maintenance management.
          for jumper usage.
Management indicated that connecting a
          The inspectors observed that maintenance management issued a
jumper to a hot lead and then routing it through a panel did not
          Maintenance Training Bulletin, dated April 1995, that dealt with
meet their expectations.
          jum3er usage. The bulletin stated, in part, that personnel
The inspectors reviewed several
          autlorized to use jumper wires are expected to know and use the
maintenance procedures and observed that general jumper usage and
                                                                              Enclosure 2 1
expectations for jumper usage was lacking.
In April and May 1995. the licensee conducted an extensive review
of jumper types, and jumper usage at the site. This review was
conducted as a result of a reactor scram following operator
deficiencies using jumpers. The inspectors observed that as a
result of this licensee review, several recommendations for jumper
types and jumper usage, and written expectations were developed.
Most departments held special training sessions for jumper usage
and the proper types of jumpers to be used.
Operations issued a
special procedure detailing operations management's expectations
for jumper usage.
The inspectors observed that maintenance management issued a
Maintenance Training Bulletin, dated April 1995, that dealt with
jum3er usage. The bulletin stated, in part, that personnel
autlorized to use jumper wires are expected to know and use the
Enclosure 2
1


        __     __   _ _ _ _ _ _ _ _ _ _                             ._ _       __   _         _   . _ _ ___
__
                                                                                                              i
__
          '
_ _ _ _ _ _ _ _ _ _
                                                                                                              ?
._ _
  1 ..
__
      -
_
                                                                                                              _;
_
                                                                                                              i
. _ _
  )
___
$                                                       22                                                   :
i
1 ..
?
'
-
_;
i
)
$
22
:
~
~
                                                                                                              ,
,
                  correct type.               Maintenance management informed the inspectors that             i
correct type.
                  proper jumper usage was taught in craft training and was primarily                           l
Maintenance management informed the inspectors that
  i               considered skill of the craft. This maintenance jumper error that                           !
i
j                 initiated this feedwater level transient was being reviewed for                             ;
proper jumper usage was taught in craft training and was primarily
j               human performance improvements.                                                             l
l
  1                                                                                                           i
i
  q         c. Conclusions                                                                                 ;
considered skill of the craft.
I                 The inspectors concluded that this maintenance jumper error
This maintenance jumper error that
                  demonstrated a poor work practice on the part of one individual.                             -
!
  ;               Similar jumper usage error has not been a concern and this error
j
J                 was an isolated occurrence. Reviewing this error for human
initiated this feedwater level transient was being reviewed for
j               performance improvements was appropriate.                                                   ,
;
                                                                                                              '
j
i           M5   Maintenance Staff Training and Qualification
human performance improvements.
;           MS.1 Maintenance Trainina and Qualification Review                                               ,
l
j             a.   Insoection Scooe (62707)                                                                     ,
1
                                                                                                                '
i
  .               A review of maintenance training documentation was conducted to
q
!                 verify that personnel involved in the repair and maintenance of                               :
c.
Conclusions
;
I
The inspectors concluded that this maintenance jumper error
demonstrated a poor work practice on the part of one individual.
-
;
Similar jumper usage error has not been a concern and this error
J
was an isolated occurrence.
Reviewing this error for human
j
performance improvements was appropriate.
,
'
i
M5
Maintenance Staff Training and Qualification
;
MS.1 Maintenance Trainina and Qualification Review
,
j
a.
Insoection Scooe (62707)
,
'
.
A review of maintenance training documentation was conducted to
!
verify that personnel involved in the repair and maintenance of
:
*
*
                  valves were appropriately trained and qualified. Also, the
valves were appropriately trained and qualified. Also, the
;
;
                  training and qualification recuirements for valve maintenance were
training and qualification recuirements for valve maintenance were
:                 discussed with Maintenance anc Training staff members.
:
discussed with Maintenance anc Training staff members.
i
l
b.
Observations and Findinas
.
;
A review of training documentation for mechanics was conducted by
)
i
i
l.            b.  Observations and Findinas
the inspectors.
;                A review of training documentation for mechanics was conducted by                            )
This review was conducted to determine the
i                the inspectors. This review was conducted to determine the                                     :
:
.               qualification status of personnel assigned to perform valve                                   )
.
;                 maintenance on safety-related and those non-safety-related valves
qualification status of personnel assigned to perform valve
i                 that are within the purview of the Maintenance Rule. The
)
                  mechanical maintenance training staff informed the inspectors that
;
                  the training and cualification requirements were the same for work
maintenance on safety-related and those non-safety-related valves
l                 on both safety anc non-safety-related valves. The training staff
i
j                 maintains the training and qualification status of personnel in a
that are within the purview of the Maintenance Rule.
!                 computer data base referred to as the Training Records and
The
j                 Qualification System (TRAQS).
mechanical maintenance training staff informed the inspectors that
the training and cualification requirements were the same for work
l
on both safety anc non-safety-related valves.
The training staff
j
maintains the training and qualification status of personnel in a
!
computer data base referred to as the Training Records and
j
Qualification System (TRAQS).
!
!
t                 The inspectors reviewed the following documents which provided the
t
]                 training and qualification requirements:
The inspectors reviewed the following documents which provided the
                  -
]
                          ANSI N18.1-1971:         Selection and Training of Nuclear Power Plant
training and qualification requirements:
j                         Personnel
-
;                -
ANSI N18.1-1971:
                          HNP-2-FSAR-13:         Section 13.1.3 Qualification Requirements for
Selection and Training of Nuclear Power Plant
                          Nuclear Plant Personnel and Section 13.1.3.1.16 Maintenance
j
Personnel
HNP-2-FSAR-13:
Section 13.1.3 Qualification Requirements for
-
;
Nuclear Plant Personnel and Section 13.1.3.1.16 Maintenance
'
'
l                         Personnel
l
Personnel
:
:
                                                                                        Enclosure 2
Enclosure 2
2.
2.
i
i
                                        . . _
..
-
.
. . _
_


      *
*
  .,
.,
                                        23
23
          -
-
              10AC-MGR-007-05: Personnel Qualification Requirements. Rev. 5
10AC-MGR-007-05: Personnel Qualification Requirements. Rev. 5
          -
-
              DI-MNT-11-0287N: Qualification of Maintenance Personnel. Rev. 2
DI-MNT-11-0287N: Qualification of Maintenance Personnel. Rev. 2
          The inspectors were informed during a discussion with maintenance
The inspectors were informed during a discussion with maintenance
          staff members that there were some Building and Grounds (B&G)
staff members that there were some Building and Grounds (B&G)
          personnel who were trained and qualified to perform valve packing.
personnel who were trained and qualified to perform valve packing.
          These individuals are assigned to the various performance teams.
These individuals are assigned to the various performance teams.
        .
They perform valve packing activities as well as laborer type
          They perform valve packing activities as well as laborer type
.
          work. A followup discussion with the mechanical maintenance
work. A followup discussion with the mechanical maintenance
          training staff indicated that these individuals attend a special
training staff indicated that these individuals attend a special
          course to become qualified as Valve Packing Technicians.     They are
course to become qualified as Valve Packing Technicians.
          provided training in mathematics, precision tools, torquing,
They are
          gasket replacement and valve packing. The instructions in this
provided training in mathematics, precision tools, torquing,
          special course is an excer)t from the curriculum for the mechanics
gasket replacement and valve packing. The instructions in this
          and the content of each su) ject area is the same. The successful
special course is an excer)t from the curriculum for the mechanics
          completion of this special course qualifies a B&G individual for a
and the content of each su) ject area is the same.
          Valve Packing Technician position on the Performance Team. The
The successful
          names of these individuals are entered into the TRAQS computer
completion of this special course qualifies a B&G individual for a
          data base as being qualified.
Valve Packing Technician position on the Performance Team. The
          The inspectors reviewed a sampling of MW0s associated with
names of these individuals are entered into the TRAQS computer
          mechanical work activities performed on valves by Mechanics and
data base as being qualified.
          B&G personnel. The MWO sampling included the following MW0s:
The inspectors reviewed a sampling of MW0s associated with
          -
mechanical work activities performed on valves by Mechanics and
              MWO 2-94-3430:   2B21-F013A. Replace SRV Top Works and Stump
B&G personnel. The MWO sampling included the following MW0s:
          -
-
              MWO 1-95-2627:   Prepare SRV Solenoid Valve Assembly and Stump
MWO 2-94-3430:
                          for Shipment to Wyle Laboratory                       ,
2B21-F013A. Replace SRV Top Works and Stump
                                                                                ;
-
          -
MWO 1-95-2627:
              MWO 2-95-1035:   Remove. Test. Replace / Repair RCIC Suction
Prepare SRV Solenoid Valve Assembly and Stump
                          Relief Valve                                         l
for Shipment to Wyle Laboratory
          -
,
              MWO 1-95-2942: Clean and Torque Valve IN22-F6081
-
          -
MWO 2-95-1035:
              MWO 1-96-0089:   Repack Valve Per 52CM-MME-001-0S                 I
Remove. Test. Replace / Repair RCIC Suction
'
Relief Valve
          -
-
              MWO 1-95-2934:   Inspect Valve IN22-F1114A for Packing
MWO 1-95-2942: Clean and Torque Valve IN22-F6081
                          Adjustment / Repacking
-
!         -
MWO 1-96-0089:
              MWO 2-95-3370:   Repair Galled Valve Stem on 2E11-F015B
Repack Valve Per 52CM-MME-001-0S
-
MWO 1-95-2934:
Inspect Valve IN22-F1114A for Packing
'
Adjustment / Repacking
!
-
MWO 2-95-3370:
Repair Galled Valve Stem on 2E11-F015B
:
!
-
MWO 2-95-3639:
Repair LPCI Valve 2 Ell-F015A Ball Stem / Valve
:
:
!        -
Stem Coupler
              MWO 2-95-3639:  Repair LPCI Valve 2 Ell-F015A Ball Stem / Valve
-
:                          Stem Coupler
MWO-2-94-1732:
          -
Perform Mechanical Portion of 52SV-T48-001-0S
              MWO-2-94-1732:   Perform Mechanical Portion of 52SV-T48-001-0S
,
,
!
!
i
i
                                                                    Enclosure 2
Enclosure 2
i
i
!
!
                                                        _ . . _ .
-, .
_ . , . _ , . .
. .
-
_
_ . . _ .
.__
- . _ .


    a
a
  .,
.,
                                          24
24
              -
MWO-1-94-5335:
                  MWO-1-94-5335: Repair / Replace and/or Bench Test Relief Valve
Repair / Replace and/or Bench Test Relief Valve
                              IN22-F070A
-
              -
IN22-F070A
                  MWO-1-96-1000: Repack Valve IN21-F023A
-
            The names of the persons who aerformed the work activity as listed
MWO-1-96-1000:
              in the MWO were compared to t1ose on the list of individuals
Repack Valve IN21-F023A
            qualified to perform the work activity on TRAQS. No discrepancies
The names of the persons who aerformed the work activity as listed
            were identified in this comparison.
in the MWO were compared to t1ose on the list of individuals
        c.   Conclusions
qualified to perform the work activity on TRAQS.
            Personnel who perform mechanical maintenance on safety and
No discrepancies
            non-safety-related valves are trained and qualified in accordance
were identified in this comparison.
            with the requirements of ANSI N18.1-1971. the FSAR, and other
c.
            applicable plant qualification procedures.
Conclusions
      M8   Miscellaneous Maintenance Issues (92700) (92902)
Personnel who perform mechanical maintenance on safety and
      M8.1 (Closed) VIO 50-321/96-06-04: Failure to Meet TS Surveillance
non-safety-related valves are trained and qualified in accordance
            Recuirements Prior to Withdrawal of a Control Rod While in Cold
with the requirements of ANSI N18.1-1971. the FSAR, and other
            Shutdown
applicable plant qualification procedures.
            This Violation was identified when, on two occasions, licensee
M8
            personnel withdrew a control rod with accumulator pressure below
Miscellaneous Maintenance Issues (92700) (92902)
            the TS requirement. The activities were performed for maintenance
M8.1
            purposes.
(Closed) VIO 50-321/96-06-04:
            The licensee's response was provided in correspondence dated
Failure to Meet TS Surveillance
            July 10. 1996. The response indicated that procedure
Recuirements Prior to Withdrawal of a Control Rod While in Cold
            34G0-0PS-066-05: Single Control Rod Withdrawal in Shutdown or
Shutdown
            Refueling, was revised to clarify the requirement that an
This Violation was identified when, on two occasions, licensee
            accumulator pressure of equal to or greater then 940 pounds per
personnel withdrew a control rod with accumulator pressure below
            square inch gauge (psig) must be present before any rod
the TS requirement.
            withdrawal. The inspectors reviewed the revised procedure. Based
The activities were performed for maintenance
            on the reviews by the inspectors and the actions taken by the
purposes.
            licensee, this violation is closed.
The licensee's response was provided in correspondence dated
      M8.2 (Closed) LER 50-321/96-06: Inadeauate Procedure and lack of Work
July 10. 1996.
            Coordination Result in Withdrawal of Inocerable Control Rod
The response indicated that procedure
34G0-0PS-066-05: Single Control Rod Withdrawal in Shutdown or
Refueling, was revised to clarify the requirement that an
accumulator pressure of equal to or greater then 940 pounds per
square inch gauge (psig) must be present before any rod
withdrawal. The inspectors reviewed the revised procedure.
Based
on the reviews by the inspectors and the actions taken by the
licensee, this violation is closed.
M8.2 (Closed) LER 50-321/96-06:
Inadeauate Procedure and lack of Work
Coordination Result in Withdrawal of Inocerable Control Rod
.
.
            This problem was discussed in IR 50-321.366/96-06.   No new issues
This problem was discussed in IR 50-321.366/96-06.
            were revealed by the LER. This LER is closed.
No new issues
                                                                        Enclosure 2
were revealed by the LER. This LER is closed.
Enclosure 2


                                _ _ _ . . _ ._             . . . _ _ _ _ _ _ _ _ _             . . _ _ _ .
_ _ _ . . _ ._
                                                                                                            !
. . . _ _ _ _ _ _ _ _ _
      *
. . _ _ _ .
  .,
!
                                                  25
*
                                                                                                            :
.,
                                          III. Enaineerina                                                 !
25
                                                                                                            !
:
        E2     Engineering Support of Facilities and Equipment
III. Enaineerina
                                                                                                            '
!
        E2.1 Trio and failure to Start Problems For the Unit 1 A Standby liauid
!
              Control (SLC) Pumo                                                                           ,
E2
        a.   Insoection Scooe (92903)
Engineering Support of Facilities and Equipment
                                                                                                            '
'
              The inspectors reviewed engineering activities of an investigation
E2.1 Trio and failure to Start Problems For the Unit 1 A Standby liauid
              of the 1A SLC pump tripping and failure to start. A review of the                             ;
Control (SLC) Pumo
              MW0s, work completed, procedures, and discussions with engineering
,
              personnel were conducted.
a.
        b.   Observations and Findinas
Insoection Scooe (92903)
              On January 10, during operations performance of a routine
'
              operability surveillance, the 1A SLC pump tripped. The system was
The inspectors reviewed engineering activities of an investigation
              declared ino)erable and actions to investigate the problem were                               4
of the 1A SLC pump tripping and failure to start. A review of the
              initiated. ,iaintenance found the motor overloads trip)ed.                                   !
;
              Maintenance later replaced a pump control switch and clanged the
MW0s, work completed, procedures, and discussions with engineering
              overload relay setting from 100% to 115%, per a telephone
personnel were conducted.
              conversation with engineering personrel, and in addition meggered
b.
              the pump motor. Later, operations personnel ran the pump for
Observations and Findinas
              about 20 minutes and it ran properly.
On January 10, during operations performance of a routine
              On January 12. operations began another operability surveillance
operability surveillance, the 1A SLC pump tripped.
              during which the pump did not start on three attempts.
The system was
              Maintenance personnel were contacted to investigate. A worn                                     i
declared ino)erable and actions to investigate the problem were
              control switch block was identified as the problem and was
4
              replaced. The pump then started properly.
initiated.
,iaintenance found the motor overloads trip)ed.
!
Maintenance later replaced a pump control switch and clanged the
overload relay setting from 100% to 115%, per a telephone
conversation with engineering personrel, and in addition meggered
the pump motor.
Later, operations personnel ran the pump for
about 20 minutes and it ran properly.
On January 12. operations began another operability surveillance
during which the pump did not start on three attempts.
Maintenance personnel were contacted to investigate.
A worn
i
control switch block was identified as the problem and was
replaced. The pump then started properly.
During the investigation of this problem, technicians identified
,
,
              During the investigation of this problem, technicians identified
that the overload heaters were not the size s?ecified in procedure
4            that the overload heaters were not the size s?ecified in procedure
4
:'
:
              52PM-R24-001-05: Allis Chalmers Low Voltage iCC Inspection,
52PM-R24-001-05: Allis Chalmers Low Voltage iCC Inspection,
              Revision 12. The procedure specified that the overload heaters
'
              should be size H80s, and size H78s had been installed.
Revision 12.
The procedure specified that the overload heaters
'
'
should be size H80s, and size H78s had been installed.
Maintenance personnel installed the correct heaters and later
,
,
              Maintenance personnel installed the correct heaters and later
changed the relay setting to 125%.
              changed the relay setting to 125%. Engineering personnel were
Engineering personnel were
'
'
              contacted to investigate the problem with the overload heaters and
contacted to investigate the problem with the overload heaters and
              to further investigate the SLC pump tripping problem to ensure
to further investigate the SLC pump tripping problem to ensure
              that the correct failure mechanism was identified.
that the correct failure mechanism was identified.
              The inspectors discussed the discrepancy of the installed overload
The inspectors discussed the discrepancy of the installed overload
l             heaters with respect to procedural requirements with engineering
l
!             personnel. The inspectors were informed that a work history
heaters with respect to procedural requirements with engineering
!
personnel. The inspectors were informed that a work history
review had been completed back to about 1984 and no evidence of
'
heater overload changeout was observed.
Documentation reviewed
;
did not indicate what size overload heaters should be installed or
'
'
              review had been completed back to about 1984 and no evidence of
when size H78 overload heaters were placed in the system.
              heater overload changeout was observed. Documentation reviewed
i
;
Enclosure 2
'
,
              did not indicate what size overload heaters should be installed or
              when size H78 overload heaters were placed in the system.
                                                                                                              i
,
                                                                                    Enclosure 2               !
i
i
                                                                                                              l
:
:
'
'
                                                                                                              l
.
                                  .__                   _
.__
_


  .
.
    '
'
..
..
                                                                                          i
i
                                          26                                             i
26
                                                                                        !
i
            Engineering personnel stated that at some time P the past, size             t
!
            H78s may have been the correct size. Engineering personnel did               l
Engineering personnel stated that at some time P the past, size
            not determine how the size H78 become installed in the system.
t
            Engineering also indicated that the overload relay was suspected             !
H78s may have been the correct size.
            as the cause of the problem and not the size of the overload                 t
Engineering personnel did
            heaters. Maintenance personnel replaced the overload relay. Both           i
l
            the overload heaters and the overload relay that was replaced were
not determine how the size H78 become installed in the system.
            tested by engineering and revealed that the pump motor would have           !
Engineering also indicated that the overload relay was suspected
            o)erated properly and within the expected overload condition of             i
!
            t1e pump motor.
as the cause of the problem and not the size of the overload
            During the procedure review and through discussions with
t
            engineering personnel, the inspectors observed that procedure
heaters.
            guidance for determining the correct size of overload heaters was           -
Maintenance personnel replaced the overload relay.
            not clear. Engineering personnel stated that procedure
Both
            clarifications would be recommended.
i
        c.   Conclusions
the overload heaters and the overload relay that was replaced were
                                                                                        l
tested by engineering and revealed that the pump motor would have
            The inspectors concluded that engineering personnel from NS&C             -!
!
            conducted a detailed review of the SLC pum) tripping problem and             ;
o)erated properly and within the expected overload condition of
            consider this as a positive attribute of t1e engineering                     i
i
            department effort. The inspectors also concluded that the SLC               l
t1e pump motor.
            pump tripping problem was an isolated occurrence. The inspectors
During the procedure review and through discussions with
                                                                                          -
engineering personnel, the inspectors observed that procedure
            did not consider that this installation of incorrect size overload
guidance for determining the correct size of overload heaters was
            heaters was an example of poor configuration control or
-
            contributed to the tripping problem.
not clear.
      E3   Engineering Procedures and Documentation                                   l
Engineering personnel stated that procedure
                                                                                          l
clarifications would be recommended.
      E3.1 Review of Engineering Evaluations                                           l
c.
                                                                                          !
Conclusions
        a.   InsDeCtion SCoDe (37551) (92903)
l
                                                                                        '
The inspectors concluded that engineering personnel from NS&C
            The inspectors reviewed licensee activities and engineering
-!
            evaluations completed for electrically backseating two Primary
conducted a detailed review of the SLC pum) tripping problem and
            Containment Isolation valves. The licensee electrically
;
                                                                                        ~
consider this as a positive attribute of t1e engineering
            backseated the valves in an attemat to identify and reduce the
i
            unidentified drywell leakage for Jnit 1.   Reactor Water Cleanup           .
department effort.
            (RWCU) Inboard Isolation valve 1G31-F001, and Reactor Core                 !
The inspectors also concluded that the SLC
            Isolation Cooling (RCIC) Inboard Isolation valve 1E51-F007, were           !
l
            electrically backseated on November 14 and December 27, 1996.               i
pump tripping problem was an isolated occurrence.
            respectfully.                                                               l
The inspectors
                                                                                        t
-
        b. Observations and Findinas                                                   !
did not consider that this installation of incorrect size overload
                                                                                        !
heaters was an example of poor configuration control or
            The inspectors reviewed an engineering evaluation conducted by             I
contributed to the tripping problem.
            corporate engineering and transmitted to the site by interoffice           !
E3
            correspondence, dated February 21, 1994, for Backseating of                 ;
Engineering Procedures and Documentation
                                                                      Enclosure 2       f
l
                                                                                        i
E3.1 Review of Engineering Evaluations
                                                                                        !
l
                                                                                        I
!
                                                                                        i
a.
                                                                                        >
InsDeCtion SCoDe (37551) (92903)
                                  -   -       _-   --           ---       -     _ ._
'
The inspectors reviewed licensee activities and engineering
evaluations completed for electrically backseating two Primary
Containment Isolation valves.
The licensee electrically
~
backseated the valves in an attemat to identify and reduce the
unidentified drywell leakage for Jnit 1.
Reactor Water Cleanup
.
(RWCU) Inboard Isolation valve 1G31-F001, and Reactor Core
!
Isolation Cooling (RCIC) Inboard Isolation valve 1E51-F007, were
!
electrically backseated on November 14 and December 27, 1996.
i
respectfully.
l
t
b.
Observations and Findinas
!
!
The inspectors reviewed an engineering evaluation conducted by
I
corporate engineering and transmitted to the site by interoffice
!
correspondence, dated February 21, 1994, for Backseating of
;
Enclosure 2
f
i
!
I
i
>
-
-
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-
.


-
-
    '
'
  .
.
                                    27
27
      Motor-0perated Valves (MOVs) in the Drywell. The engineering
Motor-0perated Valves (MOVs) in the Drywell. The engineering
      evaluation identified a total of 16 valves that were evaluated and
evaluation identified a total of 16 valves that were evaluated and
      included both Unit 1 and Unit 2 valves. Post backseating
included both Unit 1 and Unit 2 valves.
      inspections were identified for some valves and no inspection was
Post backseating
      identified for others. The evaluation specified the correct         !
inspections were identified for some valves and no inspection was
      maintenance procedure used for electrically backseating the valves   i
identified for others. The evaluation specified the correct
      and identified that the plant maintenance procedure used to
!
      backseat the valves currently required that the backseated valves
maintenance procedure used for electrically backseating the valves
      be disassembled and inspected for damage at the next opportunity.
i
      The evaluation also identified the actuators for both valves were
and identified that the plant maintenance procedure used to
      to be inspected for damage to thrust components.                     ;
backseat the valves currently required that the backseated valves
      The evaluation addressed valve actuator torque ratings, active
be disassembled and inspected for damage at the next opportunity.
      thrust ratings and valve thrust limit in the open direction. The     :
The evaluation also identified the actuators for both valves were
      evaluation concluded that "the backseat may be damaged on many of     1
to be inspected for damage to thrust components.
      the valves in cuestion if they are electrically backseated.           ,
;
      However, this camage is not postulated to prevent the valve from     i
The evaluation addressed valve actuator torque ratings, active
      performing its safety functions. Other valve components are not       I
thrust ratings and valve thrust limit in the open direction. The
      likely to be damaged by electrically backseating."                   '
:
      The inspectors reviewed table 7.3-1 of the Unit 1 FSAR and
evaluation concluded that "the backseat may be damaged on many of
      observed that the safety function of the valves was in the closed
the valves in cuestion if they are electrically backseated.
      direction. The safety evaluation satisfactorily addressed valve
,
      closing requirements and stated that deformation of the backseat
However, this camage is not postulated to prevent the valve from
      would not prevent the valves from closing.
i
      The inspectors also reviewed the interoffice correspondence
performing its safety functions.
      (memorandum) from site engineering to operations endorsing the
Other valve components are not
      1994 corporate engineering evaluation and identified other
I
      specific stipulations. The memorandum identified that the valves
likely to be damaged by electrically backseating."
      duty cycle was 15 minutes and provided guidance for not exceeding
'
      the duty cycle time. Also recommended was that administrative
The inspectors reviewed table 7.3-1 of the Unit 1 FSAR and
      controls be placed on a valve to inform operators that the valve
observed that the safety function of the valves was in the closed
      was backseated and to take actions to prevent thermal binding
direction.
      during cooldown. The inspectors identified a weakness with the
The safety evaluation satisfactorily addressed valve
      administrative control placed on the valves. This and other
closing requirements and stated that deformation of the backseat
      inspector identified deficiencies are discussed in section M3.2.
would not prevent the valves from closing.
      Also stipulated was that maintenance must generate or confirm the
The inspectors also reviewed the interoffice correspondence
      existence of MW0's to perform repacking of the backseated valve.
(memorandum) from site engineering to operations endorsing the
      The inspectors observed that the memorandum referenced maintenance
1994 corporate engineering evaluation and identified other
      procedure. 52GM-MNT-034-05, as the procedure used to backseat the
specific stipulations. The memorandum identified that the valves
      valves. The correct procedure reference was 51GM-MNT-034-0S.
duty cycle was 15 minutes and provided guidance for not exceeding
      The inspectors discussed with engineering whether any changes to
the duty cycle time. Also recommended was that administrative
      the valves, valve motors or actuators were made since 1994 that
controls be placed on a valve to inform operators that the valve
      affected the evaluation. Engineering personnel stated that no
was backseated and to take actions to prevent thermal binding
      changes were made that affected the previously completed
during cooldown.
      evaluation.
The inspectors identified a weakness with the
                                                                            1
administrative control placed on the valves.
                                                                Enclosure 2
This and other
                                                                            l
inspector identified deficiencies are discussed in section M3.2.
Also stipulated was that maintenance must generate or confirm the
existence of MW0's to perform repacking of the backseated valve.
The inspectors observed that the memorandum referenced maintenance
procedure. 52GM-MNT-034-05, as the procedure used to backseat the
valves.
The correct procedure reference was 51GM-MNT-034-0S.
The inspectors discussed with engineering whether any changes to
the valves, valve motors or actuators were made since 1994 that
affected the evaluation.
Engineering personnel stated that no
changes were made that affected the previously completed
evaluation.
Enclosure 2


  .
.
    -
-
.,
.,
                                          28
28
        c. Conclusions
c.
            The inspectors concluded that the engineering evaluation for
Conclusions
            electrically backseating valves located in the drywell was               ,
The inspectors concluded that the engineering evaluation for
            satisfactory. The evaluation considered plant safety and                 !
electrically backseating valves located in the drywell was
            identified actions to ensure continued system and component             !
,
            reliability. The typographical error on the procedure reference
satisfactory. The evaluation considered plant safety and
                                                                                      '
!
            in the memorandum was not a significant concern.                         j
identified actions to ensure continued system and component
      E8   Miscellaneous Engineering Issues (92700) (92903)
!
                                                                                      l
reliability. The typographical error on the procedure reference
      E8.1 (Closed) LER Licensee Event Reoort (LER) 50-321/96-14:       Incorrect   :
'
            Circuit Breaker Settina Results in Emeraency Diesel Generator             l
in the memorandum was not a significant concern.
            Beina Inocerable.                                                         l
j
            This problem was discussed in IR 50-321, 366/96-14. Sections M2.2
E8
            and E2.2, and was identified as an example of Violation
Miscellaneous Engineering Issues (92700) (92903)
            50-321. 366/96-14-03: Failure to Implement Configuration Control         i
l
            Requirements. The licensee determined during a system walkdown
E8.1
            that the overcurrent protection trip setpoint for the normal
(Closed) LER Licensee Event Reoort (LER) 50-321/96-14:
            sup}ly breaker to Motor Control Center (MCC) 1R24-S026. from the
Incorrect
            IB 1mergency Diesel Generator (EDG). was not set properly. The
:
            problem occurred as the result of a failure to incorporate
Circuit Breaker Settina Results in Emeraency Diesel Generator
            information developed in a design calculation into appropriate
l
            electrical single line drawings and plant maintenance procedures.
Beina Inocerable.
            Poor labeling for setting the breaker trip device was also a
l
            contributor. The long time delay pickup of the trip device should
This problem was discussed in IR 50-321, 366/96-14. Sections M2.2
            have been set at 450 amps but was left at 300 amps instead.       This
and E2.2, and was identified as an example of Violation
            problem made the IB EDG inoperable.
50-321. 366/96-14-03:
            The licensee promptly initiated a temporary modification to remove
Failure to Implement Configuration Control
            the largest load from this MCC and powered it from another source.
i
            The trip device installed on the Unit 1 600-volt feeder breaker to
Requirements. The licensee determined during a system walkdown
            the subject MCC was disabled, leaving the upstream 4160-volt
that the overcurrent protection trip setpoint for the normal
            feeder breaker to the MCC to provide overcurrent 3rotection.
sup}ly breaker to Motor Control Center (MCC) 1R24-S026. from the
            Additional corrective actions will be to remove tie trip devices
IB 1mergency Diesel Generator (EDG). was not set properly. The
            from the primary and alternate feeder breakers on the bus by
problem occurred as the result of a failure to incorporate
            June 15, 1997. The inspectors will review licensee activities to
information developed in a design calculation into appropriate
            complete the corrective actions, which are documented as IFI               l
electrical single line drawings and plant maintenance procedures.
            50-321/96-14-05: Restoration of IB EDG Motor Control Center.               l
Poor labeling for setting the breaker trip device was also a
            Based upon the inspectors review and licensee actions, the
contributor. The long time delay pickup of the trip device should
            issuance of an NOV and IFI. this LER is closed.                           I
have been set at 450 amps but was left at 300 amps instead.
      E8.2 (Closed) LER 50-321/96-14. Rev 1.:       Incorrect Circuit Breaker
This
            Settina Results in Emeraency Diesel Generator Beina :     nooerable.     ]
problem made the IB EDG inoperable.
            This LER was discussed in Section E8.1 of this report.       The LER     j
The licensee promptly initiated a temporary modification to remove
            corrected a date that licensee corrective actions will be                 ;
the largest load from this MCC and powered it from another source.
            completed. No new issues were revealed by this revision to the             l
The trip device installed on the Unit 1 600-volt feeder breaker to
            LER.   This LER is closed.
the subject MCC was disabled, leaving the upstream 4160-volt
                                                                          Enclosure 2
feeder breaker to the MCC to provide overcurrent 3rotection.
                                                                                      l
Additional corrective actions will be to remove tie trip devices
                                          vr- w w m           --
from the primary and alternate feeder breakers on the bus by
June 15, 1997. The inspectors will review licensee activities to
complete the corrective actions, which are documented as IFI
50-321/96-14-05:
Restoration of IB EDG Motor Control Center.
Based upon the inspectors review and licensee actions, the
issuance of an NOV and IFI. this LER is closed.
I
E8.2
(Closed) LER 50-321/96-14. Rev 1.:
Incorrect Circuit Breaker
Settina Results in Emeraency Diesel Generator Beina : nooerable.
]
This LER was discussed in Section E8.1 of this report.
The LER
j
corrected a date that licensee corrective actions will be
completed.
No new issues were revealed by this revision to the
LER.
This LER is closed.
Enclosure 2
tui
vr-
w
w
m
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- -
-
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a
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                                                                                          ---           - . __.
---
        -
-
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.
                                                                                                                \
__.
                                                                                                                ,
\\
                                                29
-
            E8.3   (Closed) IFI 321/96-07-03: Dearadation and Reolacement of Unit 2
.
                  Station Service Batterv 28 Due to Builduo of Cell Sediment.
,
                  This item addressed an observation of sediment buildup in the
29
                  cells of the Unit 2 Station Service Battery (SSB) 28. The vendor                             ,
E8.3
                  determined that the buildup was due to a curing 3rocess at the                               !
(Closed) IFI 321/96-07-03: Dearadation and Reolacement of Unit 2
                    factory. Of the 248 battery cells supplied for )oth trains of                               i
Station Service Batterv 28 Due to Builduo of Cell Sediment.
                  Unit 2. 56' cells showed signs of sediment. All of the cells were                             j
This item addressed an observation of sediment buildup in the
                    located among the 120 cells in SSB 28. At the end of the report
cells of the Unit 2 Station Service Battery (SSB) 28.
                  period sediment had not been observed in the cells of SSB 2A. The                             ,
The vendor
                    licensee has received replacement cells from the vendor.
,
                  MWO 2-96-1929 has been issued to replace all 120 cells of SSB 2B                             -
determined that the buildup was due to a curing 3rocess at the
                  during the upcoming Spring 1997 Unit 2 refueling outage. The MWO                             :
factory. Of the 248 battery cells supplied for )oth trains of
                  will be followed up as part of the inspectors * alanned outage                               ;
i
                    inspection activities. Based on the actions tacen by the
Unit 2. 56' cells showed signs of sediment. All of the cells were
                    licensee, this item is closed.
j
            E8.4   JClosed) LER 50-321/96-07:   Failed Comoonent Results in                                   i
located among the 120 cells in SSB 28. At the end of the report
                    : nadvertent Emeraency Diesel Generator Start.                                               ;
period sediment had not been observed in the cells of SSB 2A. The
                                                                                                                  '
,
                  This LER was issued on May 21, 1996, when the 1A EDG was
licensee has received replacement cells from the vendor.
                  inadvertently started.   Based on the actions taken by the
MWO 2-96-1929 has been issued to replace all 120 cells of SSB 2B
                  licensee, this item is closed.
-
            E8.5 (Closed) LER 50-321.366/96-08: Inadeouate Procedure Results in
during the upcoming Spring 1997 Unit 2 refueling outage. The MWO
                  Reactor Pressure Increase and Automatic Reactor Scram.
:
                  This problem was discussed in IR 50-321.366/96-06. The inspectors
will be followed up as part of the inspectors *
                  reviewed the revised procedure 3450-N32-001-1S: EHC Hydraulic
alanned outage
.                  System. Rev. 17. The inspectors also reviewed the previous
;
i                 revision. The inspectors observed that sections 7.3.1. System                                   .
inspection activities.
:                 Isolation With Bypass Capacity, and 7.3.2 Restoring the System to                               l
Based on the actions tacen by the
,                 Operation, had been deleted. This would preclude isolating                                     l
licensee, this item is closed.
1                 portions of the Electro Hydraulic Control (EHC) system which                                   )
E8.4
!                 caused the increase in reactor pressure. Based on the actions
JClosed) LER 50-321/96-07:
:                  taken by the licensee, this item is closed.
Failed Comoonent Results in
i
: nadvertent Emeraency Diesel Generator Start.
;
'
This LER was issued on May 21, 1996, when the 1A EDG was
inadvertently started.
Based on the actions taken by the
licensee, this item is closed.
E8.5 (Closed) LER 50-321.366/96-08:
Inadeouate Procedure Results in
Reactor Pressure Increase and Automatic Reactor Scram.
This problem was discussed in IR 50-321.366/96-06.
The inspectors
reviewed the revised procedure 3450-N32-001-1S:
EHC Hydraulic
System. Rev. 17.
The inspectors also reviewed the previous
.
i
revision.
The inspectors observed that sections 7.3.1. System
.
:
Isolation With Bypass Capacity, and 7.3.2 Restoring the System to
,
Operation, had been deleted. This would preclude isolating
1
portions of the Electro Hydraulic Control (EHC) system which
)
!
caused the increase in reactor pressure.
Based on the actions
taken by the licensee, this item is closed.
:
'
'
IV Plant Support
,
,
                                        IV Plant Support
R1
            R1    Radiological Protection and Chemistry Controls
Radiological Protection and Chemistry Controls
.                                                                                                               1
1
.
R1.1 General Radiological Controls
'
'
            R1.1 General Radiological Controls
Insoection Scone (71750)
                  Insoection Scone (71750)
'
'
                  General Health Physics (HP) activities were observed during the
General Health Physics (HP) activities were observed during the
                  report period. This included locked high radiation area doors,
report period.
                  proper radiological postings, and personnel frisking upon exiting
This included locked high radiation area doors,
                  the Radiologically Controlled Area (RCA). The inspectors made
proper radiological postings, and personnel frisking upon exiting
the Radiologically Controlled Area (RCA).
The inspectors made
i
i
                                                                                              Enclosure 2
Enclosure 2
                                                                                                                  1
.
      .   .                 .                 .               _ . _ _ _ _ _ - _ _ _ _ _
.
.
.
.
-


    -
-
.
.
  ,
,
                                        30
30
            frequent tours of the RCA and discussed radiological controls with         l
frequent tours of the RCA and discussed radiological controls with
          HP technicians and HP management.     No significant deficiencies         '
HP technicians and HP management.
          were identified.
No significant deficiencies
      R1.2 Radiological Controls                                                       j
'
      a.   Insoection Scooe (83750)                                                   l
were identified.
          Radiological controls associated with ongoing operational
R1.2 Radiological Controls
          activities were reviewed and evaluated. Controls for both routine
j
          operations and specific non-routine tasks were included in the
a.
          review     In particular. housekeeping and cleanliness, area
Insoection Scooe (83750)
          postin s radioactive waste (radwaste) container labels, and
Radiological controls associated with ongoing operational
          contro s for high radiation areas were reviewed for adequacy.
activities were reviewed and evaluated.
          Licensee controls for ongoing operations were compared against
Controls for both routine
          documented requirements in applicable sections of Technical                 i
operations and specific non-routine tasks were included in the
          Specifications (TSs). Final Safety Analysis Report (FSAR). and             l
review
          10 CFR Part 20.                                                             l
In particular. housekeeping and cleanliness, area
                                                                                      l
postin s radioactive waste (radwaste) container labels, and
          The inspectors made frequent tours of the RCAs. In addition.               l
contro s for high radiation areas were reviewed for adequacy.
          specific radiation work permit (RWP) procedural guidance and               !
Licensee controls for ongoing operations were compared against
          selected survey results were reviewed and discussed with
documented requirements in applicable sections of Technical
          responsible HP staff and supervisors. Operations and radiological
i
          controls associated with the low-level radioactive waste storage           j
Specifications (TSs). Final Safety Analysis Report (FSAR). and
          building were observed and evaluated. Controls for specific tasks           '
10 CFR Part 20.
          performed in accordance with the following RWPs were evaluated in
The inspectors made frequent tours of the RCAs.
          detail.
In addition.
          e   RWP 197-0005. Remove old obsolete drum capping equipment and
specific radiation work permit (RWP) procedural guidance and
                support work, effective January 10. 1997.
selected survey results were reviewed and discussed with
          e   RWP 097-0017. Process / ship / receive / load out/ transport
responsible HP staff and supervisors.
                radioactive materials and support work including alpha trending
Operations and radiological
                and Waste Separation and Temporary Storage Facility (WSTSF)
controls associated with the low-level radioactive waste storage
                work, effective January 10, 1997.
j
          In addition the inspectors reviewed and discussed program
building were observed and evaluated.
          guidance and results of internal exposure evaluations made by the
Controls for specific tasks
          licensee during 1996.
'
      b. Observations and Findinas
performed in accordance with the following RWPs were evaluated in
          High and locked high radiation area controls were verified to be
detail.
          implemented in accordance with TS requirements. Postings of
e
          radwaste storage areas were proper and in accordance with TS or
RWP 197-0005. Remove old obsolete drum capping equipment and
          10 CFR 20 Subpart J requirements. Overall, containers holding
support work, effective January 10. 1997.
          radwaste, contaminated materials, and equipment were labeled in
e
          accordance with 10 C.FR 20.1904 requirements.       Excluding activities
RWP 097-0017. Process / ship / receive / load out/ transport
          associated with construction of a hot tool room and an isolated
radioactive materials and support work including alpha trending
          example of trash and debris in the Unit 2 (U2) Radioactive Waste
and Waste Separation and Temporary Storage Facility (WSTSF)
                                                                          Enclosure 2
work, effective January 10, 1997.
In addition the inspectors reviewed and discussed program
guidance and results of internal exposure evaluations made by the
licensee during 1996.
b.
Observations and Findinas
High and locked high radiation area controls were verified to be
implemented in accordance with TS requirements.
Postings of
radwaste storage areas were proper and in accordance with TS or
10 CFR 20 Subpart J requirements.
Overall, containers holding
radwaste, contaminated materials, and equipment were labeled in
accordance with 10 C.FR 20.1904 requirements.
Excluding activities
associated with construction of a hot tool room and an isolated
example of trash and debris in the Unit 2 (U2) Radioactive Waste
Enclosure 2
--
.
.
.
.-.


              .
    .
      '
.
.
  ,
.
                                                                                l
.
                                    31
'
        (RW) building area 164 foot (*) elevation floor, cleanliness and
,
        housekeeping within the RCAs. outside radwaste ]rocessing and
l
        storage areas, and the low-level waste storage Juilding were
31
        acceptable. Radiation control activities associated with ongoing
(RW) building area 164 foot (*) elevation floor, cleanliness and
        radwaste processing, storage and shipping operations were adequate
housekeeping within the RCAs. outside radwaste ]rocessing and
        and conducted in accordance with applicable RWPs and procedures.
storage areas, and the low-level waste storage Juilding were
        During facility tours, the inspectors observed several poor
acceptable.
        radiological control practices associated with demolition of a
Radiation control activities associated with ongoing
        concrete wall located in the Unit 1 (U1) RW area 132' elevation.         '
radwaste processing, storage and shipping operations were adequate
        Demolition activities were in preparation for construction of a
and conducted in accordance with applicable RWPs and procedures.
        hot tool room and were performed under RWP 197-0005. Remove Old         ;
During facility tours, the inspectors observed several poor
        Obsolete Drum Capping Equi) ment and Support Work. effective
radiological control practices associated with demolition of a
        January 10.197       The wort area was roped-off equipped with a
'
        step-off pad, cad posted as a Contaminated Area. On                     !
concrete wall located in the Unit 1 (U1) RW area 132' elevation.
        January 15. 1997, the ins)ectors noted that the demolition
Demolition activities were in preparation for construction of a
        activities generated visi)le and potentially contaminated dust
hot tool room and were performed under RWP 197-0005. Remove Old
        which subsequently became airborne and also covered the step-off
Obsolete Drum Capping Equi) ment and Support Work. effective
        pad and areas surrounding the posted area. The only established
January 10.197
        engineering control provided was use of a High Efficiency
The wort area was roped-off equipped with a
        Particulate Air (HEPA) filtered portable exhaust ventilation             i
step-off pad, cad posted as a Contaminated Area. On
        system but without an enclosure surrounding the work area. The
!
        most recent quantitative contamination and air sample survey
January 15. 1997, the ins)ectors noted that the demolition
        results conducted on January 11, 1997, verified contamination on         l
activities generated visi)le and potentially contaminated dust
        the wall. approximately 1000 to 3000
which subsequently became airborne and also covered the step-off
                                          2
pad and areas surrounding the posted area.
                                                disintegration per minute per   l
The only established
        100 centimeters square (dpm/100cm     ) but did not identify an
engineering control provided was use of a High Efficiency
        airborne hazard. However, the inspectors noted that no additional
Particulate Air (HEPA) filtered portable exhaust ventilation
        airborne surveys were conducted within the work area and that the
i
        most recent quantitative radiation surveys completed on
system but without an enclosure surrounding the work area. The
        January 13. 1997, were in response to unexpectedly elevated
most recent quantitative contamination and air sample survey
        electronic dosimeter readings.                                           !
results conducted on January 11, 1997, verified contamination on
        Discussions with responsible HP and maintenance personnel
the wall. approximately 1000 to 3000 disintegration per minute per
        indicated that the tools used for the demolition changed and that
l
        the staff was aware of the increased levels of potentially
2
        contaminated dust outside of the designated area. Licensee
100 centimeters square (dpm/100cm ) but did not identify an
        representatives stated that additional gross contamination surveys
airborne hazard.
        of the floor conducted outside of the posted area using Masslin
However, the inspectors noted that no additional
        cloth were conducted but not documented. Responsible HP personnel
airborne surveys were conducted within the work area and that the
        stated that the gross surveys did not indicate any contamination
most recent quantitative radiation surveys completed on
        outside of the roped-off area. TS 5.4 requires that written
January 13. 1997, were in response to unexpectedly elevated
        procedures be established implemented, and maintained covering
electronic dosimeter readings.
        activities delineated in Appendix A of Regulatory Guide (RG) 1.33.
!
        Rev. 2. dated February 1978. Regulatory Guide 1.33. Appendix A.
Discussions with responsible HP and maintenance personnel
        " Typical Procedures for Pressurized Water Reactor and Boiling
indicated that the tools used for the demolition changed and that
        Water Reactors." Paragraph 7.e. requires radiation protection
the staff was aware of the increased levels of potentially
        procedures for Radiation Work Permit System and for Contamination
contaminated dust outside of the designated area.
        Control. Health Physics procedure 60AC-HPX-004-0S, Radiation and
Licensee
        Contamination Control. Revision (Rev.) 14. effective October 15,
representatives stated that additional gross contamination surveys
        1996, specifies that HP will:   initiate controls, e.g..
of the floor conducted outside of the posted area using Masslin
                                                                    Enclosure 2
cloth were conducted but not documented.
                                                                                L
Responsible HP personnel
stated that the gross surveys did not indicate any contamination
outside of the roped-off area. TS 5.4 requires that written
procedures be established implemented, and maintained covering
activities delineated in Appendix A of Regulatory Guide (RG) 1.33.
Rev. 2. dated February 1978.
Regulatory Guide 1.33. Appendix A.
" Typical Procedures for Pressurized Water Reactor and Boiling
Water Reactors." Paragraph 7.e. requires radiation protection
procedures for Radiation Work Permit System and for Contamination
Control.
Health Physics procedure 60AC-HPX-004-0S, Radiation and
Contamination Control. Revision (Rev.) 14. effective October 15,
1996, specifies that HP will:
initiate controls, e.g..
Enclosure 2
L
-
-
-


                                                                _ ___ _ _             _ _.
_ ___ _ _
    *
_
_.
*
.
.
32
l
engineering controls, to ensure that spread of contamination is
minimized; will perform non-routine radiation and contamination
surveys as required, to support operation and maintenance: will
-
perform airborne su veys during radioactive work which is expected
to cause airborne radioactivity unless constant air monitors are
,
provided: and perform periodic air sampling to evaluate the
;
effectiveness of filtered ventilation used to control airborne
radioactivity. The inspectors noted that the established
engineering controls and the contamination and airborne surveys
conducted for the observed demolition activities were not in
,
accordance with the established procedure.
]
The inspectors did not identify any significant concerns regarding
;
use of the whole body counter (WBC) equipment used for in vivo
.
.
  .                                                                                        :
analyses and results.
                                      32
Excluding concerns identified for WBC
                                                                                            l
calibration guidance detailed in Paragraph R7.1. the applicable
          engineering controls, to ensure that spread of contamination is
licensee procedures were determined to be satisfactory and staff
          minimized; will perform non-routine radiation and contamination
knowledge adequate to implement the current program.
          surveys as required, to support operation and maintenance: will                  -
Potential
          perform airborne su veys during radioactive work which is expected
procedural enhancements discussed with responsible licensee
          to cause airborne radioactivity unless constant air monitors are                ,
representatives included:
          provided: and perform periodic air sampling to evaluate the                      ;
improved guidance for evaluating
          effectiveness of filtered ventilation used to control airborne
;
          radioactivity. The inspectors noted that the established
potential internal exposure resulting from non-gamma-emitting
          engineering controls and the contamination and airborne surveys
i
          conducted for the observed demolition activities were not in                      ,
radionuclides; collection methods for bioassay sam)les and
          accordance with the established procedure.
associated vendor capabilities; and inclusion of t1e standup WBC,
                                                                                            ]
t
          The inspectors did not identify any significant concerns regarding                ;
currently used for qualitative (screening) analyses, in the
          use of the whole body counter (WBC) equipment used for in vivo                    .
crosscheck program.
          analyses and results. Excluding concerns identified for WBC
Results of all )ositive internal ex)osures of
          calibration guidance detailed in Paragraph R7.1. the applicable
workers analyzed in 1996 were less tlan one percent of tie Annual
          licensee procedures were determined to be satisfactory and staff
Limits of Intake (ALIs) documented in 10 CFR Part 20.
          knowledge adequate to implement the current program. Potential
'
          procedural enhancements discussed with responsible licensee
c.
          representatives included: improved guidance for evaluating                       ;
Conclusions
          potential internal exposure resulting from non-gamma-emitting                     i
Radiological controls for high and locked high radiation areas
          radionuclides; collection methods for bioassay sam)les and
were maintained in accordance with TS requirements. Area postings
          associated vendor capabilities; and inclusion of t1e standup WBC,                 t
and container radiation labels were appro)riate. Housekeeping and
          currently used for qualitative (screening) analyses, in the                       l
cleanliness were adequate.
          crosscheck program. Results of all )ositive internal ex)osures of
In general, t1e licensee was
          workers analyzed in 1996 were less tlan one percent of tie Annual
controlling internal exposure effectively.
          Limits of Intake (ALIs) documented in 10 CFR Part 20.
The poor engineering
                                                                                            '
controls and survey practices observed were identified as an
      c. Conclusions
example of VIO 50-321, 366/96-15-05: Failure to Follow Procedures
          Radiological controls for high and locked high radiation areas
for Contamination Control and for Deficiency Card Issuance for
          were maintained in accordance with TS requirements. Area postings
Inadequate Bioassay Calibration Guidance.
          and container radiation labels were appro)riate. Housekeeping and
R5
          cleanliness were adequate. In general, t1e licensee was
Staff Training and Qualifications in Radiation Protection and
          controlling internal exposure effectively. The poor engineering
Chemistry
          controls and survey practices observed were identified as an
a.
          example of VIO 50-321, 366/96-15-05: Failure to Follow Procedures
Insoection Scone (83750)
          for Contamination Control and for Deficiency Card Issuance for
General employee training provided to meet the requirements of
          Inadequate Bioassay Calibration Guidance.
10 CFR Part 19. and specific training and medical certification.
      R5 Staff Training and Qualifications in Radiation Protection and
required by 10 CFR Part 20 for persons who used or were designated
          Chemistry
to wear respiratory protective equipment. were reviewed and
      a. Insoection Scone (83750)
evaluated during the onsite inspection.
          General employee training provided to meet the requirements of
Enclosure 2
          10 CFR Part 19. and specific training and medical certification.
          required by 10 CFR Part 20 for persons who used or were designated
          to wear respiratory protective equipment. were reviewed and
          evaluated during the onsite inspection.
                                                                          Enclosure 2


    *
*
,
,
  ,
,
                                        33
33
            Selected 1996 training and medical certification records for
Selected 1996 training and medical certification records for
            selected personnel within the following groups were reviewed and
selected personnel within the following groups were reviewed and
          discussed with responsible licensee representatives.-
discussed with responsible licensee representatives.-
          e    Personnel evaluated by the licensee for potential internal
Personnel evaluated by the licensee for potential internal
                exposure during 1996.
e
          e   All licensee and contract personnel involved in the transfer of
exposure during 1996.
                a full radwaste liner from the radwaste processing facilities
e
                to a shipping cask during the week of January 13. 1997.
All licensee and contract personnel involved in the transfer of
          e   All contract personnel involved with routine operations at the
a full radwaste liner from the radwaste processing facilities
                low-level radioactive waste storage building.
to a shipping cask during the week of January 13. 1997.
      b. Observations and Findinas
e
          The inspectors verified that general employee and respiratory
All contract personnel involved with routine operations at the
          protection training, and medical certifications were conducted in
low-level radioactive waste storage building.
          accordance with training procedure 73TR-T-RN-001-0S General
b.
          Employee Training Programs. Rev. 9. effective June 1. 1996. The
Observations and Findinas
          guidance met the requirements of 10 CFR 19.13 and 10 CFR 20.1703.
The inspectors verified that general employee and respiratory
          Review and discussion of training records verified that all
protection training, and medical certifications were conducted in
            )ersonnel met the required general employee training requirements.
accordance with training procedure 73TR-T-RN-001-0S General
            rom review of training records and selected Respirator Device
Employee Training Programs. Rev. 9. effective June 1. 1996.
          Issuance Reports, the inspectors verified that all persons who
The
          used respiratory protection equipment were trained and medically
guidance met the requirements of 10 CFR 19.13 and 10 CFR 20.1703.
          certified in accordance with the applicable procedures.
Review and discussion of training records verified that all
      c. Conclusions
)ersonnel met the required general employee training requirements.
          General employee training and completed medical certifications for
rom review of training records and selected Respirator Device
          personnel involved in licensed activities were conducted in
Issuance Reports, the inspectors verified that all persons who
          accordance with the a)plicable procedures and met the applicable
used respiratory protection equipment were trained and medically
          requirements of 10 CFR 19 and 10 CFR 20.
certified in accordance with the applicable procedures.
      R7   Quality Assurance in Radiation Protection and Chemistry Activities
c.
      R7.1 In Vivo Ouality Control Analyses
Conclusions
      a. Insoection Scooe (83750. 84750)
General employee training and completed medical certifications for
          During the inspection, the 1996 quarterly Quality Control (OC)
personnel involved in licensed activities were conducted in
          cross-check results for the in vivo WBC quantitative (chair
accordance with the a)plicable procedures and met the applicable
          geometry) radionuclide analyses were reviewed and discussed.
requirements of 10 CFR 19 and 10 CFR 20.
      b. Observations and Findinos
R7
          For the first and fourth quarter cross-check samples, all results
Quality Assurance in Radiation Protection and Chemistry Activities
          for torso, lung and thyroid were in agreement with the vendor
R7.1
                                                                    Enclosure 2
In Vivo Ouality Control Analyses
                                                                                j
a.
Insoection Scooe (83750. 84750)
During the inspection, the 1996 quarterly Quality Control (OC)
cross-check results for the in vivo WBC quantitative (chair
geometry) radionuclide analyses were reviewed and discussed.
b.
Observations and Findinos
For the first and fourth quarter cross-check samples, all results
for torso, lung and thyroid were in agreement with the vendor
Enclosure 2
j


    -..   _     ._         ._       _ _ . _ _ _               ._._. .   . _ _         .       __.                 _.
-..
                                                                                                                        !
_
  .
._
                                                                                                                        l
._
                                                                                                                        .
_ _ . _ _ _
                                                                                                                        i
._._. .
                                                                                                                        !
. _ _
                                                              34                                                       !
.
                                                                                                                        i
__.
                          values. Disagreements between selected licensee analysis results                             i
_.
                          and the known values were identified for the second and third                                 :
!
                          cuarters of 1996. -For the second quarter samples analyzed on                                 !
l
                          Fay 23, 1996, the identified disagreements resulted from an                                   <
.
                          improper calibration conducted April 23, 1996. Responsible                                   i
.
                          licensee representatives stated that the improper calibration                                 ,
i
                          resulted from misinterpretation of calibration guidance provided                             l
!
                          by the vendor software-driven calibration menu.                                               .
34
                                                                                                                        !
!
                          From review of the applicable procedure and discus. ions with
i
                          cognizant licensee representatives, the inspectors determined that                             i
values.
                          no changes to, nor 3rocedural warnings regarding applicable                                   i
Disagreements between selected licensee analysis results
                          computer-based cali] ration menu were implemerted. A licensee                                 ;
i
                          review of.the WBC chair in vivo analysis results determined that
and the known values were identified for the second and third
                          the improper calibration had no significant effect on assignment                               l
:
                          of internal exposure for the two individuals who were evaluated                               i
cuarters of 1996. -For the second quarter samples analyzed on
                          using the WBC chair between the dates of the improper calibration                             l
!
                          and when the deficiency was identified and corrected. However,
Fay 23, 1996, the identified disagreements resulted from an
                          the inspectors noted that the subject evaluations were not
<
                          documented. The inspectors noted that RG 1.33 recommends written
improper calibration conducted April 23, 1996.
                          procedures for bioassay programs and that contrary to                                         ,
Responsible
                          administrative control procedure 10AC-MGR-004-05. Deficiency                                   l
i
                          Control System, Rev.10. dated March 3,1996, a Deficiency Card                                   i
licensee representatives stated that the improper calibration
                          for the calibration procedural inadequacy was not initiated. For
,
                          the third quarter, disagreements in results of the crosscheck
resulted from misinterpretation of calibration guidance provided
                          comparisons resulted from failure to load all the provided cross-
l
i                         check samples and did not affect the calibration accuracy.
by the vendor software-driven calibration menu.
.
!
From review of the applicable procedure and discus. ions with
cognizant licensee representatives, the inspectors determined that
i
no changes to, nor 3rocedural warnings regarding applicable
i
computer-based cali] ration menu were implemerted.
A licensee
;
review of.the WBC chair in vivo analysis results determined that
the improper calibration had no significant effect on assignment
l
of internal exposure for the two individuals who were evaluated
i
using the WBC chair between the dates of the improper calibration
l
and when the deficiency was identified and corrected. However,
the inspectors noted that the subject evaluations were not
documented.
The inspectors noted that RG 1.33 recommends written
procedures for bioassay programs and that contrary to
,
administrative control procedure 10AC-MGR-004-05. Deficiency
l
Control System, Rev.10. dated March 3,1996, a Deficiency Card
i
for the calibration procedural inadequacy was not initiated.
For
the third quarter, disagreements in results of the crosscheck
comparisons resulted from failure to load all the provided cross-
i
check samples and did not affect the calibration accuracy.
1
1
'
'
                  c.     Conclusions
c.
                          Quality control cross-check analyses were conducted in accordance
Conclusions
                          with procedural requirements. However, the failure to issue a
Quality control cross-check analyses were conducted in accordance
.                        deficiency card was identified as an additional example of
with procedural requirements.
                          procedural VIO 50-321, 366/96-15-05: Failure to Follow Procedures
However, the failure to issue a
;                         for Issuance of a Deficiency Card for Inadequate Bioassay
deficiency card was identified as an additional example of
.
procedural VIO 50-321, 366/96-15-05: Failure to Follow Procedures
;
for Issuance of a Deficiency Card for Inadequate Bioassay
Calibration Procedural Guidance.
'
'
                          Calibration Procedural Guidance.
{
{              R8         Miscellaneous Radiation Protection and Chemistry Issues
R8
l                 a.     Insoection Scooe (83750. 84750. 86750)
Miscellaneous Radiation Protection and Chemistry Issues
I                         The status of selected radiation control and radwaste performance
l
,                        indicators was reviewed and discussed with licensee
a.
j                         representatives.
Insoection Scooe (83750. 84750. 86750)
I
The status of selected radiation control and radwaste performance
indicators was reviewed and discussed with licensee
,
j
representatives.
i'
b.
Observations and Findinas
i'
i'
                  b.      Observations and Findinas
Since 1993, annual dose expenditure per unit outage continued to
i
decrease.
'
For 1996, dose expenditure was approximately 441
                          Since 1993, annual dose expenditure per unit outage continued to
person-rem and was within the established goal of 575 person-rem.
                          decrease. For 1996, dose expenditure was approximately 441
Enclosure 2
                          person-rem and was within the established goal of 575 person-rem.
,
,
                                                                                            Enclosure 2
:
:
i
i
      w -   - , , , , .     .                 .r. , ,,.,-.r         , .-
w
                                                                                -v-- , .     -       - - - - - - -
-
-
, , , , .
.
.r.
,
,,.,-.r
,
.-
-v--
, .
-
- - - - - - -


. . - - . -       -   _ .       -   -       _-- . _   _ - . _ - . - . - - - - -           .- _
. . -
< .-                                                                                               l
-
                                                                                                  i
.
                                                35
-
                  For 1996, licensee representatives informed the inspectors that no               I
-
                  abnormal effluent releases were identified. The 1996 dose                       !
_ .
                  estimates from both liquid and gaseous effluents were small                     l
-
                  percentages of the Offsite Dose Calculation Manual (ODCM) limits.               l
-
                  No significant trends or changes in radiological environmental                   i
_-- . _
                  monitoring program sample radiological analyses were identified.                 l
_ - . _ - . -
                                                                                                  !
. - - - - -
              c. Conclusions                                                                     j
.- _
                  Radiation protection performance indicators verified that licensee               ;
.-
                  actions to control worker dose were effective and radiological                   ;
<
                  effluent releases were minimized.                                               j
i
            R8.1 (Closed) Insoector Followuo Item (IFI) 50-321. 366/95-05-01:                     -
35
                  Review Post Accident Samolina System (PASS) Proaram Enhancements.               [
For 1996, licensee representatives informed the inspectors that no
                  This item was opened pending completion of equipment modifications
I
                  and procedural changes identified for the PASS system by the                     !
abnormal effluent releases were identified.
                  licensee. From selected comparison of installed PASS equipment                   ,
The 1996 dose
                  with configuration control documents arid review of current                     j
!
                  procedures, the inspectors verified completion of modifications                 ,
estimates from both liquid and gaseous effluents were small
                  and procedural revisions. On January 16, 1997, the inspectors                   ;
l
                  observed licensee representatives successfully demonstrate PASS                 ;
percentages of the Offsite Dose Calculation Manual (ODCM) limits.
                  operability by collecting, processing, and analyzing a U2 reactor                 l
l
                  coolant system (RCS) liquid sample in accordance with Chemistry                   )
No significant trends or changes in radiological environmental
                  (CH) Sampling (SAM) procedure 64CH-SAM-020-0S, Rev. 1.           From
i
                  review of selected August 1996 through January 1997 PASS In-Line
monitoring program sample radiological analyses were identified.
                  Analyses records and discussions with the licensee, the ins)ectors
l
                  verified that both containment air and RCS samples from bot 1 U1
!
                  and U2 were collected and processed by chemistry personnel using
c.
                  the PASS equipment on a routine basis. Excluding several
Conclusions
                  instances of low RCS pH determinations relative to reference
j
                  samples, no other analysis accuracy issues were identified. The
Radiation protection performance indicators verified that licensee
                  licensee stated that a review of the low pH values would be
;
                  conducted. As of November 1996. PASS availability was listed as
actions to control worker dose were effective and radiological
                  95 percent in licensee maintenance records. Based on licensee
;
                  actions and current system reliability. this item is closed.
effluent releases were minimized.
            R8.2 (Closed) Unresolved Item (URI) 50-321. 366/96-14-07: Determine if
j
                  Certificate of Comoliance (C0C) and Associated Vendor Documents
R8.1
                  for Packaae No. USA /5805/B() Were Controlled in Accordance with
(Closed) Insoector Followuo Item (IFI) 50-321. 366/95-05-01:
                  Administrative Procedure 20AC-ADM-003-05. Vendor Manual Review and
-
                  Control.
Review Post Accident Samolina System (PASS) Proaram Enhancements.
                  During review of C0Cs and associated documentation for package
[
                  type USA /5805/B() used for an August 7, 1996 Type B shipment of
This item was opened pending completion of equipment modifications
                  irradiated hardware to a licensed burial facility, the inspectors
and procedural changes identified for the PASS system by the
                  determined that current manuals and procedures were received
!
                  directly by the radaaste staff from the vendor. However, the
licensee.
                  inspectors noted that the subject documents may not have been
From selected comparison of installed PASS equipment
                                                                                  Enclosure 2
,
j
with configuration control documents arid review of current
procedures, the inspectors verified completion of modifications
,
and procedural revisions.
On January 16, 1997, the inspectors
;
observed licensee representatives successfully demonstrate PASS
;
operability by collecting, processing, and analyzing a U2 reactor
coolant system (RCS) liquid sample in accordance with Chemistry
(CH) Sampling (SAM) procedure 64CH-SAM-020-0S, Rev. 1.
From
review of selected August 1996 through January 1997 PASS In-Line
Analyses records and discussions with the licensee, the ins)ectors
verified that both containment air and RCS samples from bot 1 U1
and U2 were collected and processed by chemistry personnel using
the PASS equipment on a routine basis.
Excluding several
instances of low RCS pH determinations relative to reference
samples, no other analysis accuracy issues were identified. The
licensee stated that a review of the low pH values would be
conducted. As of November 1996. PASS availability was listed as
95 percent in licensee maintenance records.
Based on licensee
actions and current system reliability. this item is closed.
R8.2
(Closed) Unresolved Item (URI) 50-321. 366/96-14-07:
Determine if
Certificate of Comoliance (C0C) and Associated Vendor Documents
for Packaae No. USA /5805/B() Were Controlled in Accordance with
Administrative Procedure 20AC-ADM-003-05. Vendor Manual Review and
Control.
During review of C0Cs and associated documentation for package
type USA /5805/B() used for an August 7, 1996 Type B shipment of
irradiated hardware to a licensed burial facility, the inspectors
determined that current manuals and procedures were received
directly by the radaaste staff from the vendor. However, the
inspectors noted that the subject documents may not have been
Enclosure 2


  ..-   .- - - - .   .   --         . ---     .   . -     .-     - .   -     - . -
..-
u           *
.- - -
  ,
-
      ,,                                                                                      j
.
                                                                                              :
.
                                                36
--
                                                                                              i
.
                    reviewed and controlled in accordance with the applicable
---
                    administrative procedure, and thus may not have met the intent of         i
.
                    10 CFR 70.113 quality assurance (0A) requirements for shipping
. -
                    program activities. A review of licensee records identified that
.-
                    the C0C and procedures were maintained in accordance with the
-
                    applicable administrative procedure. However, the licensee was
.
                    unable to demonstrate that the subject manual was received.               !
-
                    reviewed, processed, and maintained in accordance with the subject
- .
                    administrative control procedure. All other documents associated
-
                    with shi) ping containers which were, or could be used to make             ,
u
                    Type B slipments were maintained in accordance with the licensee *s
j
                    procedure.                                                                 1
*
                    Prior to the current inspection. the licensee requested all
,,
                    uncontrolled copies of C0Cs. and associated documents from staff
,
                    members involved in transportation activities. The inspectors
:
                    reviewed a January 7.1997, letter confirming that a single copy
36
                    of shipping container documents would be sent to the licensee.
i
                    Consistent with Section IV of the Enforcement Policy based on             !
reviewed and controlled in accordance with the applicable
                    corrective actions taken prior to the end of the inspection, this         i
administrative procedure, and thus may not have met the intent of
                    issue was identified as Non-cited Violation (NCV)                         t
i
                    50-321, 366/96-15-06: Failure to Maintain Shipping Cask Manuals in         !
10 CFR 70.113 quality assurance (0A) requirements for shipping
                    Accordance with Established Procedures to Meet 10 CFR Part 70.113.
program activities. A review of licensee records identified that
                52 Status of Security Facilities and Equipment                               !
the C0C and procedures were maintained in accordance with the
                    The inspectors toured the protected area and observed that the             ;
applicable administrative procedure. However, the licensee was
                    perimeter fence was intact and not compromised by erosion nor             i
unable to demonstrate that the subject manual was received.
                    disrepair. The fence fabric was secured and barbed wire was               i
!
                    angled as required by the licensee's Plant Security Program (PSP).
reviewed, processed, and maintained in accordance with the subject
                    Isolation zones were maintained on both sides of the barrier and           ;
administrative control procedure. All other documents associated
                    were free of objects which could shield or conceal an individual.         !
with shi) ping containers which were, or could be used to make
                    The inspectors observed personnel and packages entering the
,
                    protected area were searched either by special purpose detectors
Type B slipments were maintained in accordance with the licensee *s
                    or by a physical patdown for firearms, explosives and contraband.         ;
procedure.
                    Badge issuance was observed, as was the processing and escorting           ,
1
                    of visitors. Vehicles were searched, escorted and secured as               !
Prior to the current inspection. the licensee requested all
                    described in the PSP.                                                     )
uncontrolled copies of C0Cs. and associated documents from staff
                    The inspectors concluded that the areas of the PSP inspected met
members involved in transportation activities.
                    the PSP requirements.
The inspectors
                                      V. Manaaement Meetinos                                   ,
reviewed a January 7.1997, letter confirming that a single copy
                X. Review of UFSAR Commitments                                                 l
of shipping container documents would be sent to the licensee.
                    A recent discovery of a licensee operating its facility in a               i
Consistent with Section IV of the Enforcement Policy based on
                    manner contrary to the Updated Final Safety Analysis Report
!
                    (UFSAR) description highlighted the need for a special focused
corrective actions taken prior to the end of the inspection, this
                    review that compares plant practices, procedures and/or parameters
i
                                                                              Enclosure 2
issue was identified as Non-cited Violation (NCV)
                                                                                              ;
t
                                                                                              l
50-321, 366/96-15-06: Failure to Maintain Shipping Cask Manuals in
                                                                                              l
Accordance with Established Procedures to Meet 10 CFR Part 70.113.
52
Status of Security Facilities and Equipment
!
The inspectors toured the protected area and observed that the
;
perimeter fence was intact and not compromised by erosion nor
i
disrepair. The fence fabric was secured and barbed wire was
i
angled as required by the licensee's Plant Security Program (PSP).
Isolation zones were maintained on both sides of the barrier and
;
were free of objects which could shield or conceal an individual.
!
The inspectors observed personnel and packages entering the
protected area were searched either by special purpose detectors
or by a physical patdown for firearms, explosives and contraband.
;
Badge issuance was observed, as was the processing and escorting
,
of visitors.
Vehicles were searched, escorted and secured as
described in the PSP.
)
The inspectors concluded that the areas of the PSP inspected met
the PSP requirements.
V. Manaaement Meetinos
,
X.
Review of UFSAR Commitments
A recent discovery of a licensee operating its facility in a
i
manner contrary to the Updated Final Safety Analysis Report
(UFSAR) description highlighted the need for a special focused
review that compares plant practices, procedures and/or parameters
Enclosure 2
;
l
l
-
.
.


    .
.
            '
'
  k     e,
k
                                                37
e,
                  to the UFSAR description. While performing the ins)ections
37
                  discussed in this re) ort, the inspectors reviewed t1e applicable
to the UFSAR description. While performing the ins)ections
                  portions of the UFSAR that related to the areas inspected. The
discussed in this re) ort, the inspectors reviewed t1e applicable
                  inspectors verified that the UFSAR wording was consistent with the
portions of the UFSAR that related to the areas inspected. The
                  observed plant practices procedures, and/or parameters.
inspectors verified that the UFSAR wording was consistent with the
              X.1 Exit Meeting Summary
observed plant practices procedures, and/or parameters.
                  The inspectors presented the inspection results to members of the
X.1
                  licensee management-at the conclusion of the inspection on
Exit Meeting Summary
                  January 31, 1997. The licensee acknowledged the findings
The inspectors presented the inspection results to members of the
                  presented. An interim exit was conducted on January 17, 1997.
licensee management-at the conclusion of the inspection on
                  The inspectors asked the licensee whether any materials examined
January 31, 1997.
                  during the inspection should be considered proprietary. No
The licensee acknowledged the findings
                  proprietary information was identified.
presented. An interim exit was conducted on January 17, 1997.
              X.2 Refueling Outage Management Meeting
The inspectors asked the licensee whether any materials examined
                  The inspectors attended several Outage Management Meetings
during the inspection should be considered proprietary.
                  conducted at the site. Among the items discussed were: The
No
                  Fall 1997. Unit 1 outage status: the Spring 1997. Unit 2 outage
proprietary information was identified.
                  status: the Unit 2 maintenance planning update: the Unit 2 scope
X.2
                  additions: the status of outage requisitions; and the status of
Refueling Outage Management Meeting
                  design changes. The ins ectors observed that the critical path
The inspectors attended several Outage Management Meetings
                  was identified as the hi h pressure turbine modifications. A fuel
conducted at the site. Among the items discussed were: The
Fall 1997. Unit 1 outage status: the Spring 1997. Unit 2 outage
status: the Unit 2 maintenance planning update: the Unit 2 scope
additions: the status of outage requisitions; and the status of
design changes. The ins ectors observed that the critical path
was identified as the hi h pressure turbine modifications. A fuel
shuffle, and not a fuel
ff load, will be performed.
However. the
'
'
                  shuffle, and not a fuel    ff load, will be performed. However. the
visual inspection of the vessel internal core spray piping could
>
>
                  visual inspection of the vessel internal core spray piping could
impact the outage schedule.
The inspectors concluded that the
'
'
                  impact the outage schedule. The inspectors concluded that the
outage is well planned. with realistic goals, with adequate
.                outage is well planned. with realistic goals, with adequate
.
                  support.
support.
!             X.3 Management Meeting in Region II Office
!
X.3
Management Meeting in Region II Office
i
i
i                 A licensee-requested meeting was held in the Nuclear Regulatory
i
                  Commission (NRC) office in Atlanta. Georgia on January 8.1997.
A licensee-requested meeting was held in the Nuclear Regulatory
Commission (NRC) office in Atlanta. Georgia on January 8.1997.
.
.
                  The purpose of the meeting was to discuss Georgia Power Company's
The purpose of the meeting was to discuss Georgia Power Company's
!               Self-Assessment for the Hatch nuclear plant. The NRC concluded
!
Self-Assessment for the Hatch nuclear plant.
The NRC concluded
that the meeting was beneficial in that it provided a better
>
>
                  that the meeting was beneficial in that it provided a better
t
t                understanding of accomplishments and improvement initiatives at
understanding of accomplishments and improvement initiatives at
                  the Hatch facility.   A meeting summary was documented under
the Hatch facility.
                  separate correspondence dated January 9. 1997.
A meeting summary was documented under
l
l
separate correspondence dated January 9. 1997.
.
.
4
4
                                                                          Enclosure 2
Enclosure 2
  - --_
- --


  .
.
                                                                                      i
i
      *
*
,
, ..
:
38
1
,
,
  , ..
\\
                                                                                    !
PARTIAL LIST OF PERSONS CONTACTED
                                                                                    :
)
                                                                                    1
:
                                        38                                          ,
Licensee
                                                                                    \
Anderson, J., Unit Superintendent
                      PARTIAL LIST OF PERSONS CONTACTED                             )
;
                                                                                    :
Betsill, J., Operations Manager
        Licensee
!
        Anderson, J., Unit Superintendent                                           ;
Coggin
        Betsill, J., Operations Manager                                             !
C., Engineering Support Manager
        Coggin   C., Engineering Support Manager                                   i
i
        Curtis, S., Operations Support Superintendent                               !
Curtis, S., Operations Support Superintendent
        Davis D., Plant Administration Manager                                     !
!
        Fornel, P., Performance Team Manager                                       *
Davis
        Fraser, 0., Safety Audit and Engineering Review Supervisor
D., Plant Administration Manager
        Hammonds, J., Regulatory Compliance Supervisor
!
        Kirkley, W., Health Physics and Chemistry Manager
Fornel, P., Performance Team Manager
        Lewis, J., Training and Emergency Preparedness Manager
*
        Moore, C,. Assistant General Manager - Plant Support
Fraser, 0., Safety Audit and Engineering Review Supervisor
        Reddick, R., Site Emergency Preparedness Coordinator
Hammonds, J., Regulatory Compliance Supervisor
        Roberts, P., Outages and Planning Manager                                   ;
Kirkley, W., Health Physics and Chemistry Manager
        Sumner,   H., General Manager - Nuclear Plant                               !
Lewis, J., Training and Emergency Preparedness Manager
        Thompson, J., Nuclear Security Manager                                     :
Moore, C,. Assistant General Manager - Plant Support
        Tipps, S., Nuclear Safety and Compliance Manager                           >
Reddick, R., Site Emergency Preparedness Coordinator
                                                                                    ,
Roberts, P., Outages and Planning Manager
        Wells, P., Assistant General Manager - Operations
;
                                                                                    l
Sumner, H., General Manager - Nuclear Plant
                                                                                    !
!
                                                                -
Thompson, J., Nuclear Security Manager
                                                                                    '
:
                          INSPECTION PROCEDURES USED
Tipps, S., Nuclear Safety and Compliance Manager
        IP   '551: Onsite Engineering
>
        IP 90500:     Effectiveness of Licensee Controls in                         -
,
                    Identifying, Resolving, and Preventing Problems                   l
Wells, P., Assistant General Manager - Operations
        IP 61726: Surveillance Observations
l
        IP 62700: Maintenance Implementation
!
        IP 62703:     Maintenance Observations
INSPECTION PROCEDURES USED
        IP 62707: Maintenance Observations
'
        IP 71707: Plant Operations
-
        IP 71714: Cold Weather Preparations
IP
        IP 71750:     Plant Support Activities
'551: Onsite Engineering
        IP 83750: Occupational Radiation Exposure
IP 90500:
        IP 84750: Radioactive Waste Treatment and Effluent and
Effectiveness of Licensee Controls in
                    Environmental Monitoring
-
        IP 86750: Solid Radioactive Waste Management and
Identifying, Resolving, and Preventing Problems
                      Transportation of Radioactive Materials
l
        IP 92700: Onsite Follow-up of Written Reports of Nonroutine
IP 61726:
                      Events at Power Reactor Facilities
Surveillance Observations
        IP 92901: Followup - Operations
IP 62700: Maintenance Implementation
        IP 92902: Followup - Maintenance / Surveillance
IP 62703:
        IP 92903: Followup - Followup Engineering                                   I
Maintenance Observations
        IP 92904: Followup - Plant Support                                           j
IP 62707: Maintenance Observations
                                                                                      l
IP 71707:
                                                                                    I
Plant Operations
                                                                    Enclosure 2
IP 71714: Cold Weather Preparations
                                                                                      !
IP 71750:
                                          .     ._      _        _          - _.a
Plant Support Activities
IP 83750: Occupational Radiation Exposure
IP 84750:
Radioactive Waste Treatment and Effluent and
Environmental Monitoring
IP 86750: Solid Radioactive Waste Management and
Transportation of Radioactive Materials
IP 92700: Onsite Follow-up of Written Reports of Nonroutine
Events at Power Reactor Facilities
IP 92901:
Followup - Operations
IP 92902:
Followup - Maintenance / Surveillance
IP 92903:
Followup - Followup Engineering
IP 92904:
Followup - Plant Support
j
Enclosure 2
I
.
.
.
_
. .
-
.a


        _ . _ _           _       _ _ _ _ .           _ . _ _ _ _ _ . _ _ _ _ _ . _ _             _. . - _ _
_7
_ . _
_
_
_ _ _ _ .
_ . _ _ _ _ _ . _ _ _ _ _ . _ _
_.
. - _ _
,
?
s . .. '
!
39
i
ITEMS OPENED. CLOSED. AND DISCUSSED
'
Ooened
j
50-366/96-15-01
NCV Inadequate Procedures for Replacement of the
Unit 2 Drywell Hydrogen Recombiner Flow
Controller Batteries and Establishing the
j
Required Controller " Dead Band" Following
Certain Maintenance Activities identified
(Section M2.1).
j
50-321/96-15-02
VIO Maintenance Personnel Failure To Follow
Procedure During Valve backseating Activities
i
(Section M3.2).
'
50-321.366/96-15-03 IFI Resolution of RCIC and HPC1 Turbine Speed
Control Drift Units 1 and 2. respectively
;
(Section M3.3).
50-321.366/96-15-04 IFI Switchyard Maintenance and Material Condition
(Section M1.4).
50-321.366/96-15-05 VIO Failure to Follow Procedures for Contamination
Control and for Deficiency Card Issuance for
Inadequate Bioassay Calibration Guidance
(Sections R1.2 and R7.1).
l
50-321.366/96-15-06 NCV Failure to Maintain Ship)ing Cask Manuals in
accordance with Establisled Procedures to Meet
'
10 CFR Part 70.113 (Section R8.2).
!
Closed
50-366/96-15-01
NCV Inadequate Procedures for Repl6 cement of the
Unit 2 Drywell Hydrogen Recombiner Flow
,
Controller Batteries and Establishing the
,
,
  _7
Required Controller " Dead Band" Following
s . .. '                                                                                                      ?
Certain Maintenance Activities (Section M2.1).
                                                                                                              !
50-321.366/96-15-06 NCV Failure to Maintain Ship)ing Cask Manuals in
                                                                                                                l
Accordance with Establisled Procedures to Meet
                                                      39
10 CFR Part 70.113 (Section R8.2).
                                                                                                              i
50-321.366/96-14-07 URI Deteimine if Certificate of Compliance (C0C) and
                              ITEMS OPENED. CLOSED. AND DISCUSSED                                              '
Associated Vendor Documents for Package
                                                                                                                l
No. USA /5805/B() Were Controlled in Accordance
                    Ooened                                                                                      j
with Administrative Procedure 20AC-ADM-003-0S.
              50-366/96-15-01    NCV Inadequate Procedures for Replacement of the
Vendor Manual Review and Control (Section R8.2).
                                              Unit 2 Drywell Hydrogen Recombiner Flow
Enclosure 2
                                              Controller Batteries and Establishing the                        l
                                                                                                                j
                                              Required Controller " Dead Band" Following
                                              Certain Maintenance Activities identified
                                              (Section M2.1).                                                  j
              50-321/96-15-02    VIO Maintenance Personnel Failure To Follow
                                              Procedure During Valve backseating Activities                    i
                                              (Section M3.2).                                                  I
                                                                                                                !
                                                                                                                '
              50-321.366/96-15-03 IFI Resolution of RCIC and HPC1 Turbine Speed
                                              Control Drift Units 1 and 2. respectively                        ;
                                              (Section M3.3).
              50-321.366/96-15-04 IFI Switchyard Maintenance and Material Condition
                                              (Section M1.4).
              50-321.366/96-15-05 VIO Failure to Follow Procedures for Contamination                            l
                                              Control and for Deficiency Card Issuance for                      1
                                              Inadequate Bioassay Calibration Guidance                          l
                                              (Sections R1.2 and R7.1).                                        l
              50-321.366/96-15-06 NCV Failure to Maintain Ship)ing Cask Manuals in                              l
                                              accordance with Establisled Procedures to Meet                    '
                                              10 CFR Part 70.113 (Section R8.2).                              !
                    Closed
              50-366/96-15-01    NCV Inadequate Procedures for Repl6 cement of the
                                              Unit 2 Drywell Hydrogen Recombiner Flow                          ,
                                              Controller Batteries and Establishing the                        ,
                                              Required Controller " Dead Band" Following
                                              Certain Maintenance Activities (Section M2.1).
              50-321.366/96-15-06 NCV Failure to Maintain Ship)ing Cask Manuals in
                                              Accordance with Establisled Procedures to Meet
                                              10 CFR Part 70.113 (Section R8.2).
              50-321.366/96-14-07 URI Deteimine if Certificate of Compliance (C0C) and
                                              Associated Vendor Documents for Package
                                              No. USA /5805/B() Were Controlled in Accordance
                                              with Administrative Procedure 20AC-ADM-003-0S.
                                              Vendor Manual Review and Control (Section R8.2).
                                                                                        Enclosure 2


  .
.
.
      *
*
  . ..
.
                                          40
. ..
        50-321/96-14       LER Incorrect Circuit Breaker Setting
40
                                  Results in Emergency Diesel Generator Being
50-321/96-14
                                  Inoperable (Section EB.1).
LER Incorrect Circuit Breaker Setting
        50-321/96-14. R1   LER Incorrect Circuit Breaker Setting
Results in Emergency Diesel Generator Being
                                  Results in Emergency Diesel Gcnerator Being
Inoperable (Section EB.1).
                                  Inoperable (Section E8.2).
50-321/96-14. R1
        50-321.366/96-08   LER Inadequate Procedure Results in Reactor Pressure
LER Incorrect Circuit Breaker Setting
                                  Increate and Automatic Reactor Scram
Results in Emergency Diesel Gcnerator Being
                                  (Section E8.5).
Inoperable (Section E8.2).
        50-321/96-07       LER Failed Com)onent Results in Inadvertent
50-321.366/96-08
                                  Emergency )iesel Generator Start (Section E8.4).
LER Inadequate Procedure Results in Reactor Pressure
        50-321/96-07-03     IFI Degradation and Replacement of Unit 2 Station
Increate and Automatic Reactor Scram
                                  Service Battery 2B Due to Buildup of Cell
(Section E8.5).
                                  Sediment (Section E8.3).
50-321/96-07
        50-321/96-06       LER Inadequate Procedure and Lack of Work
LER Failed Com)onent Results in Inadvertent
                                  Coordination Result in Withdrawal of Inoperable !
Emergency )iesel Generator Start (Section E8.4).
                                  Control Rod (Section M8.2).
50-321/96-07-03
        50-321.366/95-05-01 IFI Review Post Accident Sampling System (PASS)
IFI Degradation and Replacement of Unit 2 Station
                                  Program Enhancements (Section R8.1).             l
Service Battery 2B Due to Buildup of Cell
        S0-321/96-06-04     VIO Failure to Meet TS Surveillance Requirements
Sediment (Section E8.3).
                                  Prior to Withdrawal of a Control Rod While in
50-321/96-06
                                  Cold Shutdown (Section M8.1).
LER Inadequate Procedure and Lack of Work
                                                                                  1
Coordination Result in Withdrawal of Inoperable
                                                                                  !
!
                                                                                  !
Control Rod (Section M8.2).
                                                                                  !
50-321.366/95-05-01 IFI Review Post Accident Sampling System (PASS)
                                                                      Enclosure 2
Program Enhancements (Section R8.1).
                                                                                  !
S0-321/96-06-04
VIO Failure to Meet TS Surveillance Requirements
Prior to Withdrawal of a Control Rod While in
Cold Shutdown (Section M8.1).
Enclosure 2


                                                                                                                  -- .
--
  *     ..   *
.
      ,
*
                                                            41
*
                                                LIST OF ACRONYMS USED                                                   l
..
                                                                                                                        l
,
                            ALARA- As Low as Reasonably Achievable                                                     ;
41
                            ALI -
LIST OF ACRONYMS USED
                                    Annual Limit of Intake                                                             i
l
                            ANSI - American National Standards Institute                                               i
l
                            B&G - Building and Grounds                                                                l
ALARA- As Low as Reasonably Achievable
                            BOST - Beginning Of Shift Training
;
                            CFR - Code of Federal Regulations
Annual Limit of Intake
                            AGM-PS- Assistant General Manager, Plant Support                                           1
ALI
                            CH   - Chemistry                                                                           ;
i
                            cm - centimeter                                                                           l
-
                            C0C - Certificate of Compliance                                                             :
ANSI - American National Standards Institute
                            CR  -
i
                                    Control Room                                                                       ;
Building and Grounds
                            *F  -   degrees Fahrenheit                                                                 j
l
                            DC  -   Deficiency Card                                                                     t
B&G
                            DG - Diesel Generator
-
                            dpm -
BOST - Beginning Of Shift Training
                                    disintegrations per minute
CFR - Code of Federal Regulations
                            ECCS - Emergency Core Cooling Systems                                                       i
AGM-PS- Assistant General Manager, Plant Support
                            EDG - Emergency Diesel Generator                                                           !
1
                            EGM -
CH
                                    Electronic Governor Motor                                                             i
- Chemistry
                            EHC -   Electro Hydraulic Control
;
                            FME - Foreign Material Exclusion
cm
                            FSAR - Final Safety Analysis Report
- centimeter
                            GPC -
l
                                    Georgia Power Company
C0C - Certificate of Compliance
                            HEPA - High-Efficiency Particulate Air Filters
:
                            HNP -
Control Room
                                    Hatch Nuclear Plant
;
                            HP - Health Physics
CR
                            HPCI - High Pressure Coolant Irjection
-
                            HRS - Hydrogen Recombiner System
degrees Fahrenheit
                            I&C -
j
                                    Instrument and Control
*F
                            IFI -
-
                                    Inspector Followup Item
Deficiency Card
                            IR -
DC
                                    Inspection Report
t
                            IST -
-
                                    Inservice Testing
DG
                            KW  -
- Diesel Generator
                                    Kilowatt
disintegrations per minute
                            KVAR - Kilovolts Ampere Reactive
dpm
                            LER - Licensee Event Report
-
                            LPCI - Low Pressure Coolant Injection
ECCS - Emergency Core Cooling Systems
                            MCC - Motor Control Center
i
                            MG - Motor Generator
EDG - Emergency Diesel Generator
                            MOV - Motor Operated Valve
!
                            MWO - Maintenance Work Order
Electronic Governor Motor
                            NCV -
i
                                    Non-Cited Violation
EGM
                            NRC - Nuclear Regulatory Commission
-
,                          NRR - Nuclear Reactor Regulation
Electro Hydraulic Control
i                           NS&C - Nuclear Safety and Compliance                                                         ,
EHC
                            ODCM - Offsite Dose Calculation Manual                                                       l
-
i                           PASS - Post Accident Sample System
FME - Foreign Material Exclusion
                            PDR -
FSAR - Final Safety Analysis Report
                                    Public Document Room
Georgia Power Company
,                            PE0 -
GPC
                                    Plant Equipment Operator
-
                            PM - Preventative Maintenance
HEPA - High-Efficiency Particulate Air Filters
Hatch Nuclear Plant
HNP
-
HP
- Health Physics
HPCI - High Pressure Coolant Irjection
HRS - Hydrogen Recombiner System
Instrument and Control
I&C
-
IFI
-
Inspector Followup Item
IR
-
Inspection Report
IST
Inservice Testing
-
Kilowatt
KW
-
KVAR - Kilovolts Ampere Reactive
LER - Licensee Event Report
LPCI - Low Pressure Coolant Injection
MCC - Motor Control Center
MG
- Motor Generator
MOV - Motor Operated Valve
MWO - Maintenance Work Order
Non-Cited Violation
NCV
-
NRC - Nuclear Regulatory Commission
NRR - Nuclear Reactor Regulation
,
i
NS&C - Nuclear Safety and Compliance
,
ODCM - Offsite Dose Calculation Manual
l
i
PASS - Post Accident Sample System
PDR
Public Document Room
-
Plant Equipment Operator
PE0
-
,
PM
- Preventative Maintenance
.
.
;                                                                                                     Enclosure 2
;
                                                                                                                          l
Enclosure 2
,
l
,
h-
h-
    -     -
-
                . - _ - - ..           . - - . -           _ , , . - , _ _ . _ - . - - _ - _ . _ , _ _              _
-
. -
- - ..
. - - . -
_ , , . - , _ _ . _ - . - - _ - _ . _ , _ _


  t
t
      "
"
    ..
..
3
3
                                    42
42
        PSIG - Pounds Per Square Inch Gauge
PSIG -
        PSP - Plant Security Program
Pounds Per Square Inch Gauge
        PSW - Plant Service Water System
PSP - Plant Security Program
        OA   - Quality Assurance
PSW - Plant Service Water System
        QC   - Quality Control
OA
        RCA - Radiologic 61 Controlled Area
- Quality Assurance
        RCS - Reactor Coolant System
QC
        RCIC - Reactor Core Isolation Cooling
- Quality Control
        Rev - Revision
RCA - Radiologic 61 Controlled Area
        RG   - Regulatory Guide
RCS - Reactor Coolant System
        RHR - Residual Heat Removal
RCIC - Reactor Core Isolation Cooling
        RHRSW- Residual Heat Removal Service Water
Rev - Revision
        RPM - Revolutions Per Minute
RG
        RPS - Reactor Protection System
- Regulatory Guide
        RR   - Reactor Recirculation
RHR - Residual Heat Removal
        RTP - Rated Thermal Power
RHRSW- Residual Heat Removal Service Water
        RW   - Radioactive Waste
RPM - Revolutions Per Minute
        RWCU - Reactor Water Clean-up
RPS - Reactor Protection System
        RWP - Radiation Work Permit
RR
        SAM - Sampling
- Reactor Recirculation
        SCBA - Self Contained Breathing Apparatus
RTP -
        SCFM - Standard Cubic Feed Per Minute
Rated Thermal Power
        SLC - Ltandby Liquid Control
RW
        SRM - Source Range Monitor
- Radioactive Waste
        SRV - Safety Relief Valve
RWCU - Reactor Water Clean-up
        SSB - Station Service Battery
RWP - Radiation Work Permit
        TRAQS- Training Record and Qualification System
SAM - Sampling
        TRM - Technical Requirements Manual
SCBA - Self Contained Breathing Apparatus
        TS   - Technical Specifications
SCFM - Standard Cubic Feed Per Minute
        Ul.U2- Unit 1. Unit 2
SLC - Ltandby Liquid Control
        UFSAR- Updated Final Safety Analysis Report
SRM - Source Range Monitor
        URI - Unresolved Item
SRV - Safety Relief Valve
        VAC - Volts Alternating Current
SSB - Station Service Battery
        VIO - Violation
TRAQS- Training Record and Qualification System
        WBC - Whole Body Counter
TRM - Technical Requirements Manual
        WSTSF- Waste Separation and Temporary Storage Facility             ,
TS
                                                                            I
- Technical Specifications
                                                                            1
Ul.U2- Unit 1. Unit 2
                                                                            1
UFSAR- Updated Final Safety Analysis Report
                                                                Enclosure 2
URI
- Unresolved Item
VAC - Volts Alternating Current
VIO - Violation
WBC - Whole Body Counter
WSTSF- Waste Separation and Temporary Storage Facility
,
Enclosure 2
}}
}}

Latest revision as of 03:55, 12 December 2024

Insp Repts 50-321/96-15 & 50-366/96-15 on 961208-970118. Violations Noted.Major Areas Inspected:Operations,Maint, Engineering & Plant Support
ML20134L091
Person / Time
Site: Hatch  Southern Nuclear icon.png
Issue date: 01/18/1997
From:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML20134L070 List:
References
50-321-96-15, 50-366-96-15, NUDOCS 9702180262
Download: ML20134L091 (46)


See also: IR 05000321/1996015

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O.S. NUCLEAR REGULATORY COMMISSION

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REGION II

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Docket Nos:

50-321, 50-366

License Nos:

DPR-57 and NPF-5

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Report No:

50-321/96-15, 50-366/96-15

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Licensee:

Georgia Power Company (GPC)

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Facility:

E. I. Hatch Units 1 & 2

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Location:

P. O. Box 439

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Baxley' Georgia 31513

Dates:

December 8, 1996 - January 18, 1997

Inspectors:

B. Holbrook. Senior Resident Inspector

E. Christnot. Resident Inspector

J. Canady. Resident Inspector

G. Kuzo. Senior Radiation Specialist (Sections

R1.2 - R8.2)~.

W. Kleinsorge Reactor Inspector (Section M1.4)

Approved by:

P. Skinner. Chief. Projects Branch 2

Division of Reactor Projects

Enclosure 2

9702190262 970213

PDR

ADOCK 05000321

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EXECUTIVE SUMMARY

Plant Hatch Units 1 and 2

NRC Inspection Report 50-321/96-15, 50-366/96-15

This integrated inspection included aspects of licensee operations,

engineering, maintenance, and plant support. The report covers a 6-week

period of resident inspection.

In addition, it includes the results of

an announced inspection by a regional Senior Radiation Specialist and a

Reactor Engineer's inspection of electrical maintenance.

Ooerations

The inspectors concluded that Unit 2 control room operator's

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demonstrated a lack of attention to detail during control room

panel walkdowns.

Operators did not observe an incorrect switch

position and a keepfill pump that had automatically started

(Section 01.2).

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The inspectors identified as a strength operations management's

proactive actions with respect to providing operator training to

correct or prevent some deficiencies (Secticn 05.1).

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The inspectors concluded that the shift of operators reviewed for

fire fighting and fire brigade leader training and qualifications

were trained and qualified for their assigned position.

Corrective lenses for o)erator use while wearing Self Contained

Breathing Apparatus (SC3A) during control room emergencies were

readily available in the control room (Sectiori 05.2).

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The inspectors concluded that plant procedures did not include

guidance for removing valves from backseat following plant

transient conditions that resulted in a reactor cooldown.

This

was identified as a weakness.

After inspector intervention, the

additional guidance and expectations provided to operators during

shift briefings were appropriate (Section M3.2).

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The inspectors concluded that the operations department

demonstrated a commitment to self assessment and a desire for

continued improvement.

Although some corrective recunmendations

contained in the self assessment were not completed, they were

under development and the completed items were thorough and

comprehensive.

The self assessments were conducted by

knowledgeable personnel (Section 07.1).

Enclosure 2

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The failure of the traveling water screen system to operate during

cold weather conditions is identified as a significant weakness in

the area of engineering.

Engineering personnel failed to identify

that the design and system configuration did not adequately ~

3rotect system components from cold weather conditions.

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iaintenance and operations personnel also failed to identify that

portions of the system were vulnerable to cold weather conditions

during their system checks and cold weather preparations

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(Section 08.1),

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Maintenance

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The ins)ectors concluded that the maintenance work activities and

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the worc review by the system engineer for the IB Emergency Diesel

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Generator (EDG) voltage regulator re) air were thorough and

performed in accordance with applica)1e procedures.

Supervisory

and engineering oversight were evident.

The inspectors also

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concluded that the EDG design function capability was not degraded

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(Section M1.2).

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The ins)ectors concluded that the maintenance activities on the

Unit 2 Reactor Core Isolation Cooling turbine identified and

corrected the problem with the fluctuations in turbine speed

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control.

Maintenance activities observed were generally thorough

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and professional.

Supervisory and engineering oversight were

evident (Section M1.3).

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The inspectors identified an Inspector Followup Item (IFI)

50-321, 366/96-15-04:

Switchyard Maintenance and Material

Condition. This was due to the switchyard housekeeping and

material condition discrepancies and the number and age of the

predictive maintenance backlogged items for the switchyard

(Section M1.4).

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As demonstrated by good performance, the level of 3reventive

maintenance for the Reactor Protection System and Reactor

Recirculation System Motor Generator Sets was appropriate for the

circumstances (Section M1.4).

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The lack of records that support differences from equipment

manufacturers'

3reventive maintenance recommendations and

dependance on t1e collective memory of personnel was not a good

practice (Section M1.4).

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Leaving loose conductive material in electrical panels was

identified as a poor work practice for foreign material exclusion

control with the potential of shorting out components.

Some

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housekeeping discrepancies were noted (Section M1.4).

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Enclosure 2

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The inspectors identified Non-Cited Violation (NCV)

50-366/96-15-01:

Inadequate Procedures for Replacement of the

Unit 2 Drywell Hydrogen Recombiner Flow Controller Batteries and

Establishing the Required Controller " Dead Band" Following Certain

Maintenance Activities (Section M2.1).

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Operator performance during surveillance activities for the High

Pressure Coolant Injection System and EDG was generally

professional and competent. The inspectors had observed some

improvements in communications in the recent past but observed

that operations * standards were not met by all crews

(Section M3.1)

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The inspectors identified Violation (VIO) 50-321/96-15-02:

Maintenance Personnel Failure To Follow Procedure During Valve

Backseating Activities. This failure to follow procedure was

generally administrative in nature (Section M3.2).

The inspectors also concluded that some maintenance personnel's

lack of understanding of different types of procedure usage and

implementation demonstrated a weakness (Section M3.2).

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The inspectors concluded that the maintenance procedure for

electrically backseating valves did not fully implement the

requirements of the engineering evaluation. The inspectors

concluded that this deficiency did not result in a

safety-significant concern for the backseated valves

(Section M3.2).

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Inspector Followup Item (IFI) 50-321. 366/96-15-03:

Resolution of

Reactor Core Isolation Cooling (RCIC) and High Pressure Coolant

Injection System (HPCI) Turbine Speed Control Drifting, for

Units 1 and 2. respectively, was identified. The inspectors

concluded that the maximum speed drift observed on the both

systems did not affect the safety function of either system.

The

inspectors concluded that the speed control drifting could be an

indication of pending failures (Section M3.3).

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The inspectors concluded that the Unit 2 loss of feedwater heating

transient on January 5. due to a jumper grounding error,

demonstrated a poor work practice on the part of one individual.

This problem was identified as an isolated occurrence and not a

generic concern. Reviewing this error for human performance

improvements was appropriate (Section M4.1).

Personnel who perform mechanical maintenance on safety and non-

safety related valves were trained and qualified in accordance

with the requirements of ANSI N18.1-1971, the Final Safety

Analysis Report, and other applicable plant qualification

procedures (Section M5.1).

Enclosure 2

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The inspectors concluded that the Unit 1 Standby Liquid Control

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(SLC) pump tripping was an isolated problem. The inspectors

concluded that engineering personnel from the Nuclear Safety And

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Compliance (NS&C) conducted a detailed review of the SLC pump

tripping problem, and was viewed as a positive attribute of the

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department. Replacement of the system components was appropriate

(Section E2.1).

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The inspectors concluded that the engineering evaluation for

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electrically backseating valves located in the drywell was

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satisfactory. The evaluation considered plant safety and

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identified actions to ensure continued system and component

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reliability (Section E3.1).

Plant Suooort

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The inspectors identified a Violation 50-321, 366/96-15-05:

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Failure to Follow Procedures for Contamination Control and for

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Deficiency Card Issuance for Inadequate Bioassay Calibration

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Guidance. Quality control cross-check analyses were conducted in

accordance with procedural requirements (Sections R1.2 and R7.1).

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General employee training and completed medical certifications for

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personnel involved in licensed activities were conducted in

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accordance with the anlicable procedures and met the requirements

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of 10 CFR 19 and 10 C 120 (Section R.5).

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Radiation protection performance indicators verified that licensee

actions to control worker dose were effective and radiological

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effluent releases were minimized (Section R8).

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The inspectors concluded that the inspected areas of the security

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program met the applicable requirements (Section S2).

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The inspectors attended various Outage Management Meetings held at

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the site and concluded that the critical path for the refueling

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outage was identified and that the refueling outage appeared to be

well planned, with realistic goals and adequate support

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(Section X.2).

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Enclosure 2

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Reoort Details

Summary of Plant Status

Unit 1 operated at 100% rated thermal power (RTP) throughout the report

period, except for routine testing activities.

Unit 2 began the report period at 100% RTP. On January 5, power was

reduced to about 93.5% RTP due to a feedwater heater isolation.

Power

was returned to 100% RTP on the same day and operated at this power level

throughout the remainder of the report period, except for routine testing

activities.

I. Operations

01.

Conduct of Operations

01.1 General Comments (71707)

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The inspectors conducted frequent reviews of ongoing plant

operations.

In general, the conduct of operations was

are detailed in the sections below. pecific events and observation

professional and safety-conscious: s

01.2 Control Room Panel Walkdown

a.

Insoection Scooe (71707)

On January 10. the ins)ectors conducted a control room panel

walkdown of Unit 2.

T1e walkdown included safety- and

non-safety-related equipment valve lineups, switch positions and

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process instrument indications.

b.

Observations and Findinos

The inspectors observed that both keepfill pumps on the B loop of

Residual Heat Removal System (RHR) were in service.

One control

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switch was in run and the standby pump control switch was in auto.

This observation was brought to the attention of the control board

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operator.

The operator indicated that the B loop of RHR had been

in service for torus cooling during previous surveillance

activities and had been secured earlier that day, following the

completion of the surveillance activities. Tne operator indicated

that securing the RHR pump may have caused a small pressure surge

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that initiated the automatic start of the standby keepfill pump.

The operator secured the standby pump and system pressure remained

satisfactory.

The inspectors also observed that the by) ass selector switch for

the A Source Range Monitor (SRM) was in )ypass.

This was brought

to the attention of the control board operator.

The operator

Enclosure 2

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stated that the A SRM instrument cabinet had been removed from the

control room panel on January 9. for Instrumentation and Control

~ I&C) work activities. The SRM instrument cabinet had been

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replaced on the previous shift

The SRM bypass selector switch

had not been returned to normal.

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The inspectors brought these deficiencies to the attention of

operations' management for resolution.

Management's expectations

are in part, that the operators walkdown the control room front

panels once per hour and back panels once per two hours and look

for changing trends and incorrect switch positions.

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c.

Conclusions

The inspectors did not consider these deficiencies to be an

immediate concern for plant safety.

The inspectors concluded that

control room operators demonstrated a lack of attention to detail

during control room panel walkdowns. Operators failed to observe

an incorrect switch position and a keepfill pump that had

automatically started.

05

Operator Training and Qualification

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05.1 Review of ooerator "Just in Time" Trainina

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a.

Insoection Scooe (71707)

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A new training initiative, entitled "Just in Time" training

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commenced to address previous problems associated with activities

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that would affect operators.

Operations' management began "Just

in Time" training sessions for 03erators due to previous problems

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with reverse power trips of the EDGs during surveillance

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activities.

On December 26. the inspectors observed two sessions

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of "Just In Time" training for EDG manipulations during

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surveillance activities.

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b.

Observations and Findinas

The inspectors observed that the "Just in Time" training was

conducted on the plant simulator.

One session provided an

o)erator the opportunity to review the procedure and manipulate

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surveillance. prior to performing an inplant Unit 2 EDG

t1e switches

The other training session provided a different

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operator the same opportunity prior to performing a Unit 1 EDG

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surveillance.

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The inspectors observed that the training sessions were self

directed by the operators and required very little instructor

assistance. The operators reviewed the apolicable procedures and

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Enclosure 2

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performed the necessary manipulations to complete the

surveillances.

The inspectors discussed with operations' management if training

on the simulator, which is modeled after Unit 2. may present

additional challenges to operator performance when performing

Unit 1 activities.

Operations' management indicated no and

stated that, even though the simulator was modeled for Unit 2 any

switch manipulation practice would be of benefit to the operators.

c.

Conclusions

The inspectors concluded that operations' management was proactive

with respect to providing operators training to correct or prevent

some deficiencies by the "Just In Time" training.

The inspectors

observed that the "Just in Time" training was not a formal or

proceduralized process; however, operators or super isors may

request training at their discretion.

05.2 00erator Fire Briaade trainina and Qualification

a.

Inspection Scooe 71707

The inspectors reviewed fire training requirements and

qualifications for a shift of operations aersonnel. The review

was conducted for fire fighters and fire ]rigade leaders.

b.

Observations and Findinas

The inspectors reviewed the licensee's Training Records and

Qualification System Matrix Report and confirmed that operators on

shift were indicated as qualified for their fire fighting

positions.

The inspectors also verified that the operators had

successfully completed the required initial and requalification

training to maintain their qualifications.

The inspectors also verified that corrective lenses were available

in the control room for operators' use during emergencies that may

require SCBAs to be worn.

The inspectors observed that six

operators that required corrective lenses license restriction did

not have corrective eye glasses stored in the designated storage

location in the control room. The inspectors were informed by

operations supervision that the six operators wore contact lenses

instead of eye glasses.

The inspectors reviewed ap)licable

procedures that dealt with wearing contact lenses w111e wearing a

SCBA and concluded that the procedures and training were adequate.

Enclosure 2

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c.

Conclusions

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The inspectors concluded that the shift of operators reviewed for

fire fighting and fire brigade leader training and qualifications

were trained and qualified for their assigned position.

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Operators' corrective lenses for use while wearing a SCBA. during

control room emergencies, were readily available in the control

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room.

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Quality Assurance in Operations

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07.1 Licensee Self-Assessment Activities (40500)

a.

Insoection Scooe 40500

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The inspectors reviewed two licensee self assessments and followup

actions and a new procedure for Team Observations.

b.

Observations and Findinas

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The inspectors reviewed a self assessment for operations

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activities with respect to reactivity controls.

Following

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operator errors during refueling activities, control rod movement

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errors, and inattention to detail, the licensee initiated a self

assessment to identify root causes and recommend corrective

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actions.

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The inspectors reviewed the licensee's completed actions with

respect to implementing the recommendations.

The inspectors

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observed that 7 of 20 recommendations were not completed.

However, the licensee's documentation indicated that the remaining

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open items would be com eted prior to the Unit 2 refueling outage

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scheduled for March 199

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The inspectors reviewed an operations department self assessment

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completed on about September 26, 1996 that focused on identifying

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needed enhancements and generating corrective action

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recommendations aimed at hel)ing the department achieve its goal

of excellent performance.

T1e assessment was conducted at the

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request of operations' management and conducted by personnel both

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within and outside the parent organization.

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The inspectors observed that the assessment included safety focus.

management involvement, problem identification, problem

resolution, quality of operations, programs and procedures, and

operations efficiencies.

The inspectors also observed that the

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assessment provided specific observations and recommendations.

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The inspectors also reviewed procedure DI-0PS-59-0896N:

Team

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Observations. Revision 0, and observed that the procedure provided

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Enclosure 2

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a means of observing and reinforcing the operations department's

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expectations by performing supervisory and peer evaluations on

routine tasks.

Checklists for specific activities were included

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and contained a method of identifying whether or not the

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expectations were met.

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The inspectors reviewed some completed observations, checklists.

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and comments and discussed them with operation's management.

Operations' management stated that the process was still being

improved and a revision of the procedure was being developed.

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c.

Conclusions

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The inspectors concluded that the operations department

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demonstrated a commitment to self assessment and a desire for

continued improvement. Although some corrective recommendations

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were not com)leted, they were under development and the completed

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items were t1orough and comprehensive. The self assessments were

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conducted by knowledgeable personnel.

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08

Miscellaneous Operations Issues

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08.1 Cold Weather Followuo and Walkdown

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a.

Insoection Scooe (71714)(92901)

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The inspectors performed a walkdown of systems and plant

structures during hard freeze warnings.

b.

Observation and Findinas

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The inspectors observed the following during the walkdown:

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Two of the four wall manual louvers in the Fire Pump House were

not closed completely. The louvers were o

The manual roof vent was also open. pen approximately one

inch.

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Three heat trace indicating lights were not illuminated. Two

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were on the fire protection water system and the other was on

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the cooling water to the IB EDG.

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Several automatic louvers in the EDG rooms were not completely

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closed as required.

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The inspectors found from that some deficiencies still existed

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that had been previously observed as documented in

IR 50-321. 366/96-14.

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Following a hard freeze warning on about December 21. Plant

Equipment Operators (PE0) could not get the up-river or the down-

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Enclosure 2

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river traveling water screens to operate.

Subsequent trouble

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shooting by maintenance personnel identified that the pressure

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switches for both screens had frozen. The inspectors observed the

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pressure switch installations and observed that the sensing lines

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to the switches were heat traced, but a problem existed in that

switches were not heat traced or insulated in order to read their

indication. Maintenance personnel corrected this problem and

later enclosed the switches with insulating material, installed

heat lamas and directed the lamps toward the pressure switches. A

design clange was initiated to make permanent repairs.

The inspectors were informed that operations personnel had tested

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the traveling screens due to information received from industry

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experience.

Freezing problems with traveling screens had been

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identified at other sites.

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The inspectors found from the reviews and discussions with

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licensee personnel that the traveling water screen system for both

units would not operate in manual or automatic due to the pressure

switch problem. As a result, the support systems affecting plant

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safety systems, such as Plant Service Water (PSW) and Residual

Heat Removal Service Water "lHRSW). were not available during this

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cold weather condition. The licensee's prompt corrective actions

restored the function of the pressure switches. The affected

plant safety systems would have performed their required

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functions.

c.

Conclusions

The inspectors concluded that the deficiencies obser ved during the

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walk downs were not significant for the existing outside

temperatures and the cleanliness of the river water and river

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level at the time of the walk downs.

Maintenance and operations

personnel failed to identify that portions of the system were

vulnerable to cold weather conditions during their system checks

and cold weather preparations.

Engineering personnel failed to

identify that the design and system configuration did not

adequately protect system components from cold weather conditions.

The failure of the traveling water screen system to operate during

cold weather conditions is identified as a significant weakness in

the area of engineering.

Enclosure 2

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II. Maintenance

M1

Conduct of Maintenance

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M1.1 General Comments

a.

Insoection Scooe (62707)

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The inspectors observed all or portions of the following work

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MWO 1-96-4722:

Electrically backseat RCIC Inboard

Isolation Valve 1E51-F007

MWO 1-96-4362:

Electrically backseat RWCU Inboard

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Isolation Valve 1G31-F001

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MWO 2-96-3361: Repair 1B EDG Auto Voltage Regulator

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MWO 2-96-0042: Repair Unit 2 RCIC EGM Control Box

MWO 2-96-2976:

Repair Unit 2 RCIC Data Input to DAAS

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MWO 1-97-0066:

Investigate Tripping of 1A SLC Pump

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MWO 1-97-0071:

Replace Overload Heaters in 1A SLC Pump

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MWO 1-97-0092:

Replace Overload Relay for 1A SLC Pump

b.

Observations and Findinas

The inspectors found that the work was performed in accordance

with actively used work packages. Appro)riate post modification

and maintenance tests were performed. Tlese tests consisted of

operating the equipment following the completion of work

activities.

Additional inspector observations are documented in Sections M1.2

and M1.3.

M1 -. 2 Reoairs to 1B EDG Automatic Voltaae Reaulator

a.

Insoection Scone (62707)

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The inspectors observed work activities performed on the IB

Emergency Diesel Generator (EDG) automatic voltage regulator under

Maintenance Work Order (MWO) 2-96-3361. The inspectors discussed

the activities with maintenance, engineering and operations

personnel.

b.

Observations and Findinas

The inspectors were informed that while performing 3rocedure

34SV-R43-002-2S: Diesel Generator IB Monthly Test

Rev.18, with

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voltage regulation in automatic control and the voltage at 4120

volts alternating current (VAC), the voltage could not be adjusted

Enclosure 2

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to the required 4160 VAC. The automatic voltage adjustment must'

be performed at the local panel due to the design of the system.

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Troubleshooting activities discovered defective diodes in the

direct current drive motor circuit of the voltage regulator. The

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motor positions the automatic regulator rheostat which sets the

voltage level for automatic control. The inspectors discussed the

failure of the diodes with engineering personnel and were informed

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that the motor and rheostat were seldom exercised and this may

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have contributed to the failure.

The system engineer indicated

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that a recommendation to exercise the motor and rheostat more

often would be made.

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During the repair activities. the inspectors observed that the new

diodes were installed by craft personnel using applicable

procedures with supervisory and engineering oversight. Subsequent

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to the repair, a new motor-rheostat unit was installed and the

repaired unit was returned to the warehouse as a spare.

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The inspectors were informed by engineering that the EDG would

have controlled the voltage in automatic at 4120 VAC instead of

4160 VAC and the difference in voltage was not enough to affect

safety-related loads.

c.

Conclusion

Maintenance activities observed were generally thorough and

professional.

Supervisory and engineering oversight were evident.

The inspectors concluded that the work activities and the review

by the sy'. tem engineer for the IB EDG voltage regulator were

thorough and performed in accordance with applicable procedures.

The inspectors also concluded that the EDG was capable of

performing the required safety functions.

M1.3 Reoairs to Unit 2 Reactor Core Isolation Coolino (RCIC) Turbine

Soeed Control

a.

Insoection Scone (62707)

The inspectors reviewed the results of the maintenance activities

and observed the post maintenance test of the Unit 2 RCIC turbine.

The system had been declared inoperable due to speed control

problems.

b.

Observations and Findinos

The activities were performed under MW0s 2-96-0042 and 2-96-2976.

and ap)licable procedures.

Trouble shooting activities indicated

that tie electronic governor motor (EGM) was defective. The EGM

Control Box was replaced and the RCIC was satisfactorily tested.

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Enclosure 2

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The defective electronic governor was bench tested and confirmed

that the trouble shooting findings were correct.

Inspector

observations on the Unit 2 RCIC post maintenance and operability

testing are documented in Section M3.3 of this report.

c.

Conclusions

Maintenance activities observed were generally thorough and

professional. Supervisory and engineering oversight were evident.

The ins)ectors concluded that the maintenance activities on the

Unit 2 RCIC identified and corrected the 3roblem with the

fluctuations in turbine speed control. T1e two reversed wires

discovered did not affect system operability but demonstrated a

lack of attention to detail.

M1.4 Electrical Maintenance Imolementation

a.

Insoection Scooe (62700)

To evaluate electrical maintenance implementation as it relates to

motor generator (MG) sets and switchyard equipment, the inspectors

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conducted: walkdown inspections of the Reactor Protection System

(RPS) and Reactor Recirculation System (RR) MG set rooms and

selected areas of the switchyards and the switchyard control

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house; and reviews of equipment manufacturers' technical manuals.

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re)etitive task records, maintenance records, and oil analysis and

vi) ration test data.

The inspectors compared the equipment

manufacturers' maintenance recommendations with the licensee's

maintenance program for both scope and periodicity.

b.

Observations and Findinas

Reactor Protection System and Reactor Recirculation System MG Sets

Housekeeping was good with the following exceptions:

o

A number of structural fasteners were missing from control

panels.

The concern was that the missing fasteners could

abrogate the seismic qualification of the pariels.

e

The closure devices on a number of panel doors were not secured

such that the weather stripping was compressed.

The concern

was that the improper sealing of the panels could abrogate the

environmental qualification.

e

Metal shavings (probably the debris left from drilling) and

miscellaneous fasteners were found adrift inside control

panels.

Leaving loose conductive material in electrical panels

was identified as a poor work practice control with the

Enclosure 2

.

_ _ _ _

. _ . _

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.

,

10

potential of shorting out components.

The fasteners were

removed by the licensee,

e

The Reactor Recirculation System MG set oil circulation systems

leak.

To address this issue, the licensee conducts daily wipe

downs and was actively pursuing a permanent repair.

There was a number of areas where the liccnsee's repetitive

preventive maintenance program was not consistent with the

<

equipment manufacturer's recommendations. The licensee was unable

)

to provide documented justifications for the differences.

i

However, the licensee was able to provide anecdotal information

j

remembered by maintenance personnel that supported the deviations.

>

Records, examined by the inspectors. reflected that repetitive

preventive maintenance activities were completed within the

scheduled time period.

I

Records reflect that the repetitive preventive maintenance program

!

'

had been effective as few repetitive corrective maintenance

i

activities were required.

l

i

Switchyards

Maintenance in the switchyards was performed by Georgia Power

Company Transmission Maintenance Center with procedures issued by

l

l

the Transmission Operation and Maintenance Manager.

Some

j

surveillances were performed by Plant Hatch Operations Department

l

personnel.

Ins)ection of housekeeping and material condition revealed a

I

num)er of items that needed attention.

Protective coatings on

4

l

exterior equipment had deteriorated, as evidenced by many areas of

)

l

rust and missing closure fasteners.

Inside the switch house, the

inspectors noted un-taped spare electrical leads in the back board

i

area, trash, and evidence of feline habitation.

Conductive

material (metal shavings and fasteners) was found in both exterior

l

<

panels and in the back board area in the switch house.

The

'

fasteners were removed on the spot. The effectiveness of rain

,

gutters on the switch house was minimal in deflecting water away-

t

i

from the structure, due to advanced corrosion.

l

l

There was a number of areas where the licensee's repetitive

maintenance program for switchyard equipment was not consistent

!

with the equipment manufacturer's recommendations. The licensee

'

was unable to 3rovide documented justifications for the

!

differences,

iowever, the licensee was able to provide anecdotal

.

information, remembered by Transmission Maintenance Center

personnel, that supported the differences.

l

3

Enclosure 2

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<

Transmission Maintenance Center records reflected that there were

,

19 repetitive maintenance tasks that were overdue, the oldest of

which had a due date of July 23, 1992.

The overdue activities

were various 3reventative diagnos11c tests of air blast breakers.

Transmission iaintenance Center records were such that timeliness

.

of completed maintenance tasks could not be determined.

!

c.

Conclusions

'

As demonstrated by good performance, the level of 3reventive

maintenance for the Reactor Protection System and Reactor

Recirculation System Motor Generators (MG) was a?propriate for the

4

circumstances.

Some housekeeping discrepancies were noted. The

,

lack of records that support differences from equipment

I

manufacturer's areventive maintenance recommendations, and

dependance on t1e collective memory of personnel was not a good

practice.

Due tc the switchyard housekee)ing and material condition

discrepancies identified and tie number and age of the predictive

maintenance backlogged items, switchyard maintenance will be the

subject of a future NRC inspection. This matter will be

identified as Inspector Followup Item 50-321, 366/96-15-04:

Switchyard Maintenance and Material Condition.

'

M2

Maintenance end Material Condition of Facilities and Equipment

!

'M2.1

Hydroaen Recombiner Unit 2

a.

Insoection Scooe (92902)

.

!

On November 21. 1996, the ins)ectors observed that an 18-month

surveillance for the Unit 2A )rywell Hydrogen Recombiner System

-

(HRS) could not be performed to due problems with inlet valve.

2T49-F003A. The controller for the valve was not operating

3roperly. The inspectors reviewed past performance and work

listory for the system. The system had been declared inoperable

so that corrective maintenance could be completed.

i

'

b.

Observations and Findinas

The inspectors reviewed documentation dated from November 20

,

to 24, concerning the HRS and observed the following:

1

-

On November 20. the HRS 2A, Panel 2T49-P600A was removed from

i

service for testing of motor operated valves (MOVs) and the

i

replacement of MOV electrical overloads

Enclosure 2

, , - ,

.-.y

.,

,.

,,

-

.

m

u,

.a__._..uua-.m

.__..___,.2

w.,

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12

On November 21, the surveillance for the HRS valve operability

l

-

was satisfactorily completed and the recombiner functional test

]

was started at 3:30 a.m.

-

On November 21. at 5:20 p.m., a functional test was

unsatisfactory due to a controller memory loss for inlet

'

MOV 2T41-F003A. The loss of memory was due to a loss of power.

The controller loses power when the breaker for the MOV is

<

racked out.

-

On November 22 problems continued with valve 2T41-F003A. The

valve cycled partially open and closed and technicians were

concerned that the motor on the valve would overheat, causing

damage. The gain on the controller was adjusted with no affect

and engineering personnel continued their investigation.

Licensee documentation revealed the problem was corrected and the

2A HRS was returned to service at 11:45 p.m. on November 24.

The inspectors identified from reviews and discussions with

f

licensee personnel the following:

the batteries located in the

'

flow controllers have a service life of five years, and a shelf

life of about three to four years, according to vendor

information: the batteries had not been changed since Unit 2 was

licensed in 1978: and the batteries were installed in order to

protect the controllers from a loss of programming during a loss

,

of power.

The inspectors also identified that no procedure discussed the

batteries, required that they be functionally tested, nor that

they be changed in accordance with vendor recommendations.

EDG

3ersonnel responsible for the system failed to ensure that the

l

3attery replacement was specified in plant procedures.

The inspectors were later informed that, following maintenance

activities on the valve a controller " dead band" was required to

,

be established for proper operation of the valve and valve

controller.

This requirement was also not identified in any

,

procedure, post maintenance testing, or calibration activity.

l

t

When the maintenance activities on the valve were completed. I&C

l

completed the required calibrations and the old battery was

>

tested.

It satisfactorily performed.

Since the licensee did not

!

have a spare battery, the old one was left in place.

The licensee

i

initiated procurement activities to purchase a new battery.

.

The inspectors verified that procedures were revised to identifv

I

~

establishing the require " dead band" following maintenance or

i

calibration activities. The inspectors verified that procedures

Enclosure 2

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13

were scheduled to be revised to include replacing the battery

within the required vendor recommended frequency.

c.

Conclusions

The inspectors concluded from reviews and discussion with licensee

personnel that the Unit 2 Drywell HRS flow controller batteries

exceeded the vendor recommended service life.

Procedures were

inadequate in that battery replacement was not identified.

Additionally, the procedures were inadequate for establishing the

required valve controller " dead band" following certain

maintenance activities. This violation constitutes a violation of

minor safety significance and is being identified as

NCV 50-366/96-15-01:

Inadequate Procedures for Replacement of the

Unit 2 Drywell Hydrogen Recombiner Flow Controller Batteries and

Establishing the Required Controller " Dead Band" Following Certain

Maintenance Activities, consistent with Section IV of the NRC

Enforcement Policy.

M3

Maintenance Procedures and Documentation

M3.1 Surveillance Observations

a.

Insoection Scooe (61726)

The inspectors observed all or portions of the following Unit 1

and Unit 2 surveillance activities:

- 345V-E41-002-15: HPCI Pump Operability.. Revision (Rev.) 19

- 34SV-R43-001-1S: DG 1A Monthly Test, Rev. 17. ED 1

- 34SV-E41-002-2S: HPCI Pump Operability. Rev. 23

- 34SV-E51-002-1S:

RCIC Pump Operability. Rev. 17

- 34SV-E51-002-2S:

RCIC Pump Operability. Rev. 16

b.

Observations and Findinas

On December 26, the inspectors attended the pre-job briefing in

preparation for the Unit 1 High Pressure Core Injection (HPCI)

surveillar,ce activities and observed operator actions during

portions of the surveillance.

The test was also >erformed to meet

the Inservice Testing (IST) requirements for the iPCI system.

The

inspectors observed that a member of engineering su) port,

maintenance, health physics (HP), o)erations and t1e system

engineer were present at the pre-jo) briefing.

The Assistant

General Manager - Plant Support (AGM-PS) was present for the

majority of the briefing.

During the briefing, operations personnel requested that HP ensure

j

that no personnel were in the torus area.

This was for personnel

protection, based upon previous industry operating event history

Enclosure 2

J

,-

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I

14

i

for failure of small turbine exhaust diaphragms.

HP personnel

ensured that no personnel were in the area and posted it.

The inspectors observed that hydrogen injection was lowered to

about 8 standard cubic feed per minute (SCFM) and that the

applicable technical requirements manual (TRM) action statement

for the main steam line radiation monitors being set

non-conservatively was entered.

3

The inspectors observed that a HP technical was present locally

and had identified the HPCI room as a High radiation area. A

minimal number of personnel entered the HPCI room during

operation, consistent with As low As Reasonably Achievable (ALARA)

considerations. Maintenance and other personnel were on standby

at a designated low dose area.

The inspectors observed that operator actions in the control room

were adequate. Appropriate attention to detail, procedural usage,

and supervisory oversight were demonstrated. Communications were

not all 3-part, but did not present any observable problems during

The i'spectors discussed operator

the surveillance.

n

communications during the surveillance and general communications

with operations * management. Operations * management stated that a

j

renewed emphasis had been placed on communications and that some

crews demonstrated better communications than others.

The inspectors toured the EDG building and observed the 1A EDG

during the surveillance run. The inspectors identified a small

oil leak on the governor that had not been previously identified.

The leak was brought to the attention of operators stationed at

the EDG who contacted maintenance personnel, who repaired the

leak

c.

Conclusions

The Unit 1 HPCI and EDG systems performed as required and met the

ap)licable TS criteria.

However, the HPCI pump outboard bearing

vi) ration increased to the alert range. requiring that the

surveillance test frequency for HPCI pump be doubled.

The

performance of the operators and crews conducting the

surveillances was generally professional and competent.

The

inspectors had observed some improvements in communications in the

recent past but observed that operations * standards were not met

by all crews.

No other deficiencies were identified.

Enclosure 2

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t

H3.2 Review of Maintenance Activities to Electrically Backseat Valves.

!

a.

Insoection Scooe (62703)

The inspectors reviewed maintenance activities and documentation

i

for electrically backseating two Primary Containment Isolation

'

valves. The licensee electrically backseated the valves in an

i

attempt to identify and reduce the unidentified drywell leakage-

f

for Unit 1.

Reactor Water Cleanup (RWCU) Inboard Isolation

j

valve 1G31-F001, and RCIC Inboard Isolation valve 1E51-F007. were

!

electrically backseated on November 14 and December 27. 1996.

i

'

respectfully. The inspectors reviewed the corporate engineering

evaluation (section E3.1 of this report) to ensure that all

a>plicable actions were completed. Additional inspector

o)servations are discussed in section E3.1 of this report.

b.

Observations and Findinas.

'

The inspectors reviewed procedure 51GM-MNT-034-05:

MOV Electrical

f

Backseating With Instantaneous Circuit Breaker Trip Protection,

j

Rev. 2. The following are deficiencies that were identified by the

'

inspectors:

'

-

The Evaluation section of the corporate engineering evaluation

stated that procedure 51GM-MNT-034-05, limits the motor current

(of the valve being backseated) to twice the rated current.

However, step 7.6 of the procedure states, in part, to " adjust

breaker 2 on the backseat apparatus to 2 times rated amps

(+/- 50%)." This would allow a maximum of three times rated

motor current, not twice the motor current, as s)ecified in the

engineering evaluation.

Engineering concluded tlat this

difference was not a safety concern for the valve since the

engineering evaluation was more concerned with locked rotor

current.

-

Special requirements. Step 4.3.2 of the backseating procedure

and the engineering evaluation, states, in part, that prior to

performing backseating, the Shift Supervisor on duty will

review the engineering evaluation for the impact on stroke time

requirements and will indicate the results cf Ms review in the

work performed section of the MW0.

This documentation was not completed for either of the two

valves that were backseated. The inspectors discussed this

deficiency with maintenance and operations personnel.

The

operations supervisor on shift during one of the backseating

activities stated that he did not review the maintenance

procedure and was not aware of the documentation requirement.

The inspectors discussed maintenance activities with respect to

Enclosure 2

_

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.

.

16

reviewing procedures prior to their use and how maintenance

communicated specific requirements to operations personnel. The

inspectors were informed that if a maintenance procedure

contained specific requirements for operations personnel,

maintenance personnel were required to bring the requirement to

the attention of operations.

,

i

The inspectors reviewed procedure 10AC-MGR-019-05:

Procedure

l

Use and Adherence Rev. O, and observed that step 4.3.4,

!

stated, in part, that all plant personnel were responsible ~for

.

reviewing and understanding procedures prior to using them.

The inspectors concluded that in at least one example discussed

above, maintenance personnel responsible for the valve

backseating procedure did not bring the specific documentation

requirement to the attention of operations' supervision. The

,

inspectors noted that after bringing the deficiency to the

attention of the maintenance personnel..the documentation was

later completed.

i

During the discussion with maintenance personnel concerning

!

procedure use, the inspectors were informed that some sections

of maintenance procedures may be considered continuous use,

-

some sections may be considered reference use, and other parts

may be considered information use. The inspectors discussed

different procedure usage with at least five different

i

maintenance personnel and discovered that no clear

understanding of procedure usage was evident. The inspectors

.

reviewed Procedure 10AC-MGR-019-0S. Rev. O. and discussed

!

procedure usage with maintenance management. The inspectors

i

were informed that improvement in procedure usage continued to

be a challenge and management's expectations were not being

!

met.

,

!

It was not clear to the inspectors how some personnel's

misunderstanding of procedure usage would ensure effective and

i

consistent implementation of the procedures.

Procedure usage

j

appeared to be very subjective on the part of the user and

!

would not necessarily ensure that management's expectations for

i

procedure usage were consistently met.

The inspectors

'

concluded that maintenance personnel's understanding of

different procedure usage and implementation demonstrated a

,

weakness.

-

-

Procedure step 4.3.4 stated, in part. that the engineering

,

evaluation must be attached to Attachment 1 of the procedure

i

and filed in Document Control with a copy attached to the MWD.

The inspectors observed that during the review of the MWO work

[

package for the backseating completed on November 14 the

Enclosure 2

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17

engineering evaluation was not part of the MWO work package and

)

.

was not attached to Attachment 1.

The inspectors noted that

!

the MWO work package was being maintained open until after

outage work. After bringing this deficiency to the attention

j

of maintenance personnel. the engineering evaluation was

included as-part of the MWO package and properly attached to

i

!

the procedure.

j

.

v._adure step 4.3.5 stated. in part, that a MWO must be

i

-

initiated for internal inspection on the valve to be

i

j

backseated.

The inspectors observed that the engineering evaluation did not

l

-

specify that an internal inspection of the valve be completed.

i

.

i

However, the evaluation identified that the procedure required

an internal inspection of the valve that was backseated.

The

,

inspectors observed that a MWO was not initiated for an

internal inspection of the valve backseated on December 27.

During a discussion with the system engineer he indicated that

i

-

'

!

an internal valve inspection would be completed provided other

inspections of the valve and or actuator indicated that an

j

internal inspection was warranted.

i

For the valve backseated on November 14. the MWO identified

l

that an internal valve ins)ection be performed but referenced

an incorrect procedure.

T1e procedure referenced and

'

!

documented on the MWO did not exist.

This deficiency was

maintenance personnel. pectors identified the problem to

corrected after the ins

'

4

l

-

The engineering evaluation recommended that o)erations

implement administrative controls to ensure tlat the backseated

l

valves would be removed from backseat prior to a 100 degree

Fahrenheit ( F) cooldown of the reactor.

Operations placec

caution tags on the valves to meet this recommendation.

The inspectors observed the caution tags placed on the

i

backseated valves and noted that the caution tags stated that

the valves were electrically backseated.

The caution tag book

did not contain any additional information.

The inspectors

>

.

reviewed procedure 34G0-0PS-013-2S:

Normal Plant Shutdown.

Rev. 21. and observed that step 7.3.26 stated, in part, that

!

3rior to cooldown greater than 100 F. remove all MOVs that have

3een electrically or manually backseated from their backseat.

The procedure did not provide additional instructions for the

activity.

.

The ins)ectors discussed a concern with operations' management

as to w1 ether the operators had sufficient guidance for

,

removing valves from their backseated condition during all

,

.

Enclosure 2

i

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18

plant conditions. The normal method of removing a valve from

its backseat was to close the valve using the control room

handswitch. The inspectors concern was that if operators used

this method of removing valves from their backseat. RCIC and

RWCU system (and other systems with backseated valves) would be

isolated when they may be needed for continued safe unit

shutdown.

As a result of this discussion operations'

management provided additional instructions for the beginning

of shift training (BOST) for each operating crew informing

them of expectations and priorities during plant transient

conditions. The inspectors did not identify similar

instructions in the unit's scram proced r e.

c.

Conclusions

The inspectors concluded that failure to follow procedures

51GM-MNT-034-OS and 10 AC-MGR-019-0S by maintenance personnel to

ensure that steps were completed was a violation.

This was

identified as Violation 50-321/96-15-02: Maintenance Personnel

Failure To Follow Procedure During Valve Backseating Activities.

The inspectors concluded that maintenance personnel's lack of

understandina of the different types of procedure usage

requirements and implementation demonstrated a weakness.

The inspectors concluded that the maintenance procedure for

electrically backseating valves did not fully implement the

requirements of the engineering evaluation.

The inspectors

concluded that this deficiency did not result in a safety

significant concern for the backseated valves.

M3.3 Unit 1 RCIC and Unit 2 HPCI Soeed Control Chances

a.

Insoection Scooe (92902)

The ins)ectors observed upward drifts in the Unit 1 RCIC and

Unit 2 iPCI turbine speed controls during the 3erformance of

surveillance tests. The drifting occurred wit 1out operator

actions. The inspectors reviewed and discussed the results of the

Unit 2 RCIC test performed on January 9 with operations and

engineering personnel.

The inspectors also observed a

post-maintenance test of the Unit 2 RCIC system on January 10 (See

Section M1.3).

b.

Observations and Findinas

The inspectors observed, reviewed, and discussed the results of

the operability surveillance tests for the Unit 1 RCIC Pump and

the Unit 2 HPCI Pump.

The ins)ectors also observed maintenance

activities for the repair of t1e Unit 2 RCIC pump.

The inspectors

Enclosure 2

.m,

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'

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19

-

attended the operations pre-job and post-job briefings..

The

briefings were thorough and stressed effective communications,

procedure adherence. job assignments, responsibilities, and test

results.

The inspectors observed the following during the Unit 1 RCIC

turbine test:

-

The RCIC pump turbine was manually started and after one minute

into the test the turbine speed appeared to stabilize at about

4460 revolutions per minute (rpm), as required oy procedure

-

At approximately four minutes into the test the turbine speed

drifted up to 4500 rpm

-

The operator took control of the turbine and lowered the speed

to 4460 rpm and at eight minutes into the test the turbine

appeared to stabilize at that speed

-

At approximately 15 minutes into the test the turbine speed

started to drift up again

-

The test was completed at approximately 25 minutes and the

turbine speed had drifted up to 4490 rpm

The inspectors reviewed test results data which verified what the

ins)ectors had observed concerning the upward drift of the RCIC

tur)ine speed.

During discussions with operators and engineers,

the inspectors were informed that the Control Room (CR) turbine

speed indication was 100 rpm lower than the actual turbine speed.

The inspectors observed the following during the Unit 2 HPCI

turbine test:

The HPCI turbine was started, came up to set speed, and

-

appeared to stabilize at 3865 rpm

-

Shortly after the speed stabilized, a gradual upward drift

began. At the end of the test, which lasted for 21 minutes,

the turbine appeared to be controlling at 3910 rpm

-

The lowest rpm observed by the inspectors was 3862 and the

highest was 3918 rpm

The inspectors found from the observations, discussions and

reviews taat the upward drift of the Unit 1 RCIC turbine speed was

not expected.

The turbine speed drift should not have occurred

because of the design of the system. The system should have

stabilized around 4460 rpm instead of having a constant upward

l

Enclosure 2

j

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20

drift.

The system engineer, stationed locally at the Unit 1 RCIC

pump, assumed that the upward drift was due to operator action.

The upward drift observed on the Unit 2 HPCI turbine continued

throughout the test. The inspector discussed the observation of

the drift with operations personnel.

Licensee personnel discussed

several possibilities for the deficiencies which included out of

calibration electronics, a test valve gradually clogging up with

debris, or a mechanical malfunction of the test valve.

!

Subsequent to the Unit 1 RCIC turbine test a Unit 2 RCIC turbine

test was performed.

During the test the operators observed

i

significant changes in the speed of the Unit 2 RCIC turbine. The

I&C technicians informed the operators that the turbine control

i

'

valve was receiving full open signals followed by full closed

signals on a continuous basis.

The turbine control valve appeared

to go to the fully open position and immediately go to the fully

closed position.

This caused observed fluctuations in turbine

speed of up to plus-or-minus 160 rpm. The operators declared the

Unit 2 RCIC system inoperable.

The RCIC system engineer informed

the ins)ectors that the Unit 2 RCIC system would operate in this

manner )ut not for very long.

The inspectors observed the

post-maintenance test of the Unit 2 RCIC and did not observe any

deficiencies.

c.

Conclusions

The inspectors concluded that the maximum drift observed on the

Unit 1 RCIC turbine was 40 rpm.

The upward drift of the Unit 2

HPCI turbine was about 45 rpm. The inspectors concluded that the

drifts could be an indication of pending failures.

The erratic

speed control of the Unit 2 RCIC was a significant problem. This

was identified as IFI 50-321, 366/96-15-03:

Resolution of RCIC

and HPCI Turbine Speed Control Drift Units 1 and 2. respectively.

M4

Maintenance Staff Knowledge and Performance

M4.1

Inadvertent Feedwater Heater Isolation.

a.

Insoection Scooe (62707)

J

The inspectors conducted a review of maintenance work activities,

reviewed documentation and discussed maintenance personnel

performance with licensee personnel with respect to an inadvertent

isolation of a Unit 2 feedwater heater,

b.

Observations and Findinas

On January 5, during maintenance activities to replace a relay on

the 6th stage A heater steam trap bypass to the condenser. a fuse

Enclosure 2

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.

.

.. . - .

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21

blew.

As a result, steam from the high pressure turbine to the

6th stage heaters was isolated, causing feedwater heater levels to

become erratic.

Operators observed that feedwater temperature decreased and

entered the abnormal procedure for loss of feedwater temperature.

Power was reduced to about 93.5% RTP. The blown fuse was

replaced, heater levels were stabilized and power was later

returned to 100% RTP.

The relay, which remained in the energized

state even though the relay fuse had blown, was not immediately

replaced.

The relay was replaced the following day after a work

plan was completed by engineering and maintenance personnel. The

inspectors noted that while similar relays had failed, sticking in

the energized condition was an unusual case.

The inspectors reviewed procedure 34AB-N21-001-2S:

Loss of

Feedwater Heating. Revision 2. and observed that operators

initiated the correct actions for the plant transient.

The inspectors discussed maintenance personnel's actions involved

with the relay replacement with maintenance supervision.

The

inspectors were informed that an I&C technician was in the process

of jumpering out the relay to be replaced had connected one end

of the jumper to a hot lead, and was routing the jumper through

the panel toward the other lead that was to be jumpered.

The

jumper was inadvertently grounded blowing the fuse, and

initiating the transient.

The inspectors discussed expectations for jumper usage with

maintenance management.

Management indicated that connecting a

jumper to a hot lead and then routing it through a panel did not

meet their expectations.

The inspectors reviewed several

maintenance procedures and observed that general jumper usage and

expectations for jumper usage was lacking.

In April and May 1995. the licensee conducted an extensive review

of jumper types, and jumper usage at the site. This review was

conducted as a result of a reactor scram following operator

deficiencies using jumpers. The inspectors observed that as a

result of this licensee review, several recommendations for jumper

types and jumper usage, and written expectations were developed.

Most departments held special training sessions for jumper usage

and the proper types of jumpers to be used.

Operations issued a

special procedure detailing operations management's expectations

for jumper usage.

The inspectors observed that maintenance management issued a

Maintenance Training Bulletin, dated April 1995, that dealt with

jum3er usage. The bulletin stated, in part, that personnel

autlorized to use jumper wires are expected to know and use the

Enclosure 2

1

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correct type.

Maintenance management informed the inspectors that

i

proper jumper usage was taught in craft training and was primarily

l

i

considered skill of the craft.

This maintenance jumper error that

!

j

initiated this feedwater level transient was being reviewed for

j

human performance improvements.

l

1

i

q

c.

Conclusions

I

The inspectors concluded that this maintenance jumper error

demonstrated a poor work practice on the part of one individual.

-

Similar jumper usage error has not been a concern and this error

J

was an isolated occurrence.

Reviewing this error for human

j

performance improvements was appropriate.

,

'

i

M5

Maintenance Staff Training and Qualification

MS.1 Maintenance Trainina and Qualification Review

,

j

a.

Insoection Scooe (62707)

,

'

.

A review of maintenance training documentation was conducted to

!

verify that personnel involved in the repair and maintenance of

valves were appropriately trained and qualified. Also, the

training and qualification recuirements for valve maintenance were

discussed with Maintenance anc Training staff members.

i

l

b.

Observations and Findinas

.

A review of training documentation for mechanics was conducted by

)

i

the inspectors.

This review was conducted to determine the

.

qualification status of personnel assigned to perform valve

)

maintenance on safety-related and those non-safety-related valves

i

that are within the purview of the Maintenance Rule.

The

mechanical maintenance training staff informed the inspectors that

the training and cualification requirements were the same for work

l

on both safety anc non-safety-related valves.

The training staff

j

maintains the training and qualification status of personnel in a

!

computer data base referred to as the Training Records and

j

Qualification System (TRAQS).

!

t

The inspectors reviewed the following documents which provided the

]

training and qualification requirements:

-

ANSI N18.1-1971:

Selection and Training of Nuclear Power Plant

j

Personnel

HNP-2-FSAR-13:

Section 13.1.3 Qualification Requirements for

-

Nuclear Plant Personnel and Section 13.1.3.1.16 Maintenance

'

l

Personnel

Enclosure 2

2.

i

..

-

.

. . _

_

.,

23

-

10AC-MGR-007-05: Personnel Qualification Requirements. Rev. 5

-

DI-MNT-11-0287N: Qualification of Maintenance Personnel. Rev. 2

The inspectors were informed during a discussion with maintenance

staff members that there were some Building and Grounds (B&G)

personnel who were trained and qualified to perform valve packing.

These individuals are assigned to the various performance teams.

They perform valve packing activities as well as laborer type

.

work. A followup discussion with the mechanical maintenance

training staff indicated that these individuals attend a special

course to become qualified as Valve Packing Technicians.

They are

provided training in mathematics, precision tools, torquing,

gasket replacement and valve packing. The instructions in this

special course is an excer)t from the curriculum for the mechanics

and the content of each su) ject area is the same.

The successful

completion of this special course qualifies a B&G individual for a

Valve Packing Technician position on the Performance Team. The

names of these individuals are entered into the TRAQS computer

data base as being qualified.

The inspectors reviewed a sampling of MW0s associated with

mechanical work activities performed on valves by Mechanics and

B&G personnel. The MWO sampling included the following MW0s:

-

MWO 2-94-3430:

2B21-F013A. Replace SRV Top Works and Stump

-

MWO 1-95-2627:

Prepare SRV Solenoid Valve Assembly and Stump

for Shipment to Wyle Laboratory

,

-

MWO 2-95-1035:

Remove. Test. Replace / Repair RCIC Suction

Relief Valve

-

MWO 1-95-2942: Clean and Torque Valve IN22-F6081

-

MWO 1-96-0089:

Repack Valve Per 52CM-MME-001-0S

-

MWO 1-95-2934:

Inspect Valve IN22-F1114A for Packing

'

Adjustment / Repacking

!

-

MWO 2-95-3370:

Repair Galled Valve Stem on 2E11-F015B

!

-

MWO 2-95-3639:

Repair LPCI Valve 2 Ell-F015A Ball Stem / Valve

Stem Coupler

-

MWO-2-94-1732:

Perform Mechanical Portion of 52SV-T48-001-0S

,

!

i

Enclosure 2

i

!

-, .

_ . , . _ , . .

. .

-

_

_ . . _ .

.__

- . _ .

a

.,

24

MWO-1-94-5335:

Repair / Replace and/or Bench Test Relief Valve

-

IN22-F070A

-

MWO-1-96-1000:

Repack Valve IN21-F023A

The names of the persons who aerformed the work activity as listed

in the MWO were compared to t1ose on the list of individuals

qualified to perform the work activity on TRAQS.

No discrepancies

were identified in this comparison.

c.

Conclusions

Personnel who perform mechanical maintenance on safety and

non-safety-related valves are trained and qualified in accordance

with the requirements of ANSI N18.1-1971. the FSAR, and other

applicable plant qualification procedures.

M8

Miscellaneous Maintenance Issues (92700) (92902)

M8.1

(Closed) VIO 50-321/96-06-04:

Failure to Meet TS Surveillance

Recuirements Prior to Withdrawal of a Control Rod While in Cold

Shutdown

This Violation was identified when, on two occasions, licensee

personnel withdrew a control rod with accumulator pressure below

the TS requirement.

The activities were performed for maintenance

purposes.

The licensee's response was provided in correspondence dated

July 10. 1996.

The response indicated that procedure

34G0-0PS-066-05: Single Control Rod Withdrawal in Shutdown or

Refueling, was revised to clarify the requirement that an

accumulator pressure of equal to or greater then 940 pounds per

square inch gauge (psig) must be present before any rod

withdrawal. The inspectors reviewed the revised procedure.

Based

on the reviews by the inspectors and the actions taken by the

licensee, this violation is closed.

M8.2 (Closed) LER 50-321/96-06:

Inadeauate Procedure and lack of Work

Coordination Result in Withdrawal of Inocerable Control Rod

.

This problem was discussed in IR 50-321.366/96-06.

No new issues

were revealed by the LER. This LER is closed.

Enclosure 2

_ _ _ . . _ ._

. . . _ _ _ _ _ _ _ _ _

. . _ _ _ .

!

.,

25

III. Enaineerina

!

!

E2

Engineering Support of Facilities and Equipment

'

E2.1 Trio and failure to Start Problems For the Unit 1 A Standby liauid

Control (SLC) Pumo

,

a.

Insoection Scooe (92903)

'

The inspectors reviewed engineering activities of an investigation

of the 1A SLC pump tripping and failure to start. A review of the

MW0s, work completed, procedures, and discussions with engineering

personnel were conducted.

b.

Observations and Findinas

On January 10, during operations performance of a routine

operability surveillance, the 1A SLC pump tripped.

The system was

declared ino)erable and actions to investigate the problem were

4

initiated.

,iaintenance found the motor overloads trip)ed.

!

Maintenance later replaced a pump control switch and clanged the

overload relay setting from 100% to 115%, per a telephone

conversation with engineering personrel, and in addition meggered

the pump motor.

Later, operations personnel ran the pump for

about 20 minutes and it ran properly.

On January 12. operations began another operability surveillance

during which the pump did not start on three attempts.

Maintenance personnel were contacted to investigate.

A worn

i

control switch block was identified as the problem and was

replaced. The pump then started properly.

During the investigation of this problem, technicians identified

,

that the overload heaters were not the size s?ecified in procedure

4

52PM-R24-001-05: Allis Chalmers Low Voltage iCC Inspection,

'

Revision 12.

The procedure specified that the overload heaters

'

should be size H80s, and size H78s had been installed.

Maintenance personnel installed the correct heaters and later

,

changed the relay setting to 125%.

Engineering personnel were

'

contacted to investigate the problem with the overload heaters and

to further investigate the SLC pump tripping problem to ensure

that the correct failure mechanism was identified.

The inspectors discussed the discrepancy of the installed overload

l

heaters with respect to procedural requirements with engineering

!

personnel. The inspectors were informed that a work history

review had been completed back to about 1984 and no evidence of

'

heater overload changeout was observed.

Documentation reviewed

did not indicate what size overload heaters should be installed or

'

when size H78 overload heaters were placed in the system.

i

Enclosure 2

,

i

'

.

.__

_

.

'

..

i

26

i

!

Engineering personnel stated that at some time P the past, size

t

H78s may have been the correct size.

Engineering personnel did

l

not determine how the size H78 become installed in the system.

Engineering also indicated that the overload relay was suspected

!

as the cause of the problem and not the size of the overload

t

heaters.

Maintenance personnel replaced the overload relay.

Both

i

the overload heaters and the overload relay that was replaced were

tested by engineering and revealed that the pump motor would have

!

o)erated properly and within the expected overload condition of

i

t1e pump motor.

During the procedure review and through discussions with

engineering personnel, the inspectors observed that procedure

guidance for determining the correct size of overload heaters was

-

not clear.

Engineering personnel stated that procedure

clarifications would be recommended.

c.

Conclusions

l

The inspectors concluded that engineering personnel from NS&C

-!

conducted a detailed review of the SLC pum) tripping problem and

consider this as a positive attribute of t1e engineering

i

department effort.

The inspectors also concluded that the SLC

l

pump tripping problem was an isolated occurrence.

The inspectors

-

did not consider that this installation of incorrect size overload

heaters was an example of poor configuration control or

contributed to the tripping problem.

E3

Engineering Procedures and Documentation

l

E3.1 Review of Engineering Evaluations

l

!

a.

InsDeCtion SCoDe (37551) (92903)

'

The inspectors reviewed licensee activities and engineering

evaluations completed for electrically backseating two Primary

Containment Isolation valves.

The licensee electrically

~

backseated the valves in an attemat to identify and reduce the

unidentified drywell leakage for Jnit 1.

Reactor Water Cleanup

.

(RWCU) Inboard Isolation valve 1G31-F001, and Reactor Core

!

Isolation Cooling (RCIC) Inboard Isolation valve 1E51-F007, were

!

electrically backseated on November 14 and December 27, 1996.

i

respectfully.

l

t

b.

Observations and Findinas

!

!

The inspectors reviewed an engineering evaluation conducted by

I

corporate engineering and transmitted to the site by interoffice

!

correspondence, dated February 21, 1994, for Backseating of

Enclosure 2

f

i

!

I

i

>

-

-

_-

--

---

-

.

-

'

.

27

Motor-0perated Valves (MOVs) in the Drywell. The engineering

evaluation identified a total of 16 valves that were evaluated and

included both Unit 1 and Unit 2 valves.

Post backseating

inspections were identified for some valves and no inspection was

identified for others. The evaluation specified the correct

!

maintenance procedure used for electrically backseating the valves

i

and identified that the plant maintenance procedure used to

backseat the valves currently required that the backseated valves

be disassembled and inspected for damage at the next opportunity.

The evaluation also identified the actuators for both valves were

to be inspected for damage to thrust components.

The evaluation addressed valve actuator torque ratings, active

thrust ratings and valve thrust limit in the open direction. The

evaluation concluded that "the backseat may be damaged on many of

the valves in cuestion if they are electrically backseated.

,

However, this camage is not postulated to prevent the valve from

i

performing its safety functions.

Other valve components are not

I

likely to be damaged by electrically backseating."

'

The inspectors reviewed table 7.3-1 of the Unit 1 FSAR and

observed that the safety function of the valves was in the closed

direction.

The safety evaluation satisfactorily addressed valve

closing requirements and stated that deformation of the backseat

would not prevent the valves from closing.

The inspectors also reviewed the interoffice correspondence

(memorandum) from site engineering to operations endorsing the

1994 corporate engineering evaluation and identified other

specific stipulations. The memorandum identified that the valves

duty cycle was 15 minutes and provided guidance for not exceeding

the duty cycle time. Also recommended was that administrative

controls be placed on a valve to inform operators that the valve

was backseated and to take actions to prevent thermal binding

during cooldown.

The inspectors identified a weakness with the

administrative control placed on the valves.

This and other

inspector identified deficiencies are discussed in section M3.2.

Also stipulated was that maintenance must generate or confirm the

existence of MW0's to perform repacking of the backseated valve.

The inspectors observed that the memorandum referenced maintenance

procedure. 52GM-MNT-034-05, as the procedure used to backseat the

valves.

The correct procedure reference was 51GM-MNT-034-0S.

The inspectors discussed with engineering whether any changes to

the valves, valve motors or actuators were made since 1994 that

affected the evaluation.

Engineering personnel stated that no

changes were made that affected the previously completed

evaluation.

Enclosure 2

.

-

.,

28

c.

Conclusions

The inspectors concluded that the engineering evaluation for

electrically backseating valves located in the drywell was

,

satisfactory. The evaluation considered plant safety and

!

identified actions to ensure continued system and component

!

reliability. The typographical error on the procedure reference

'

in the memorandum was not a significant concern.

j

E8

Miscellaneous Engineering Issues (92700) (92903)

l

E8.1

(Closed) LER Licensee Event Reoort (LER) 50-321/96-14:

Incorrect

Circuit Breaker Settina Results in Emeraency Diesel Generator

l

Beina Inocerable.

l

This problem was discussed in IR 50-321, 366/96-14. Sections M2.2

and E2.2, and was identified as an example of Violation

50-321. 366/96-14-03:

Failure to Implement Configuration Control

i

Requirements. The licensee determined during a system walkdown

that the overcurrent protection trip setpoint for the normal

sup}ly breaker to Motor Control Center (MCC) 1R24-S026. from the

IB 1mergency Diesel Generator (EDG). was not set properly. The

problem occurred as the result of a failure to incorporate

information developed in a design calculation into appropriate

electrical single line drawings and plant maintenance procedures.

Poor labeling for setting the breaker trip device was also a

contributor. The long time delay pickup of the trip device should

have been set at 450 amps but was left at 300 amps instead.

This

problem made the IB EDG inoperable.

The licensee promptly initiated a temporary modification to remove

the largest load from this MCC and powered it from another source.

The trip device installed on the Unit 1 600-volt feeder breaker to

the subject MCC was disabled, leaving the upstream 4160-volt

feeder breaker to the MCC to provide overcurrent 3rotection.

Additional corrective actions will be to remove tie trip devices

from the primary and alternate feeder breakers on the bus by

June 15, 1997. The inspectors will review licensee activities to

complete the corrective actions, which are documented as IFI

50-321/96-14-05:

Restoration of IB EDG Motor Control Center.

Based upon the inspectors review and licensee actions, the

issuance of an NOV and IFI. this LER is closed.

I

E8.2

(Closed) LER 50-321/96-14. Rev 1.:

Incorrect Circuit Breaker

Settina Results in Emeraency Diesel Generator Beina : nooerable.

]

This LER was discussed in Section E8.1 of this report.

The LER

j

corrected a date that licensee corrective actions will be

completed.

No new issues were revealed by this revision to the

LER.

This LER is closed.

Enclosure 2

tui

vr-

w

w

m

w--

--

- - - -

- -

-

u-

a

-

.

---

-

.

__.

\\

-

.

,

29

E8.3

(Closed) IFI 321/96-07-03: Dearadation and Reolacement of Unit 2

Station Service Batterv 28 Due to Builduo of Cell Sediment.

This item addressed an observation of sediment buildup in the

cells of the Unit 2 Station Service Battery (SSB) 28.

The vendor

,

determined that the buildup was due to a curing 3rocess at the

factory. Of the 248 battery cells supplied for )oth trains of

i

Unit 2. 56' cells showed signs of sediment. All of the cells were

j

located among the 120 cells in SSB 28. At the end of the report

period sediment had not been observed in the cells of SSB 2A. The

,

licensee has received replacement cells from the vendor.

MWO 2-96-1929 has been issued to replace all 120 cells of SSB 2B

-

during the upcoming Spring 1997 Unit 2 refueling outage. The MWO

will be followed up as part of the inspectors *

alanned outage

inspection activities.

Based on the actions tacen by the

licensee, this item is closed.

E8.4

JClosed) LER 50-321/96-07:

Failed Comoonent Results in

i

nadvertent Emeraency Diesel Generator Start.

'

This LER was issued on May 21, 1996, when the 1A EDG was

inadvertently started.

Based on the actions taken by the

licensee, this item is closed.

E8.5 (Closed) LER 50-321.366/96-08:

Inadeouate Procedure Results in

Reactor Pressure Increase and Automatic Reactor Scram.

This problem was discussed in IR 50-321.366/96-06.

The inspectors

reviewed the revised procedure 3450-N32-001-1S:

EHC Hydraulic

System. Rev. 17.

The inspectors also reviewed the previous

.

i

revision.

The inspectors observed that sections 7.3.1. System

.

Isolation With Bypass Capacity, and 7.3.2 Restoring the System to

,

Operation, had been deleted. This would preclude isolating

1

portions of the Electro Hydraulic Control (EHC) system which

)

!

caused the increase in reactor pressure.

Based on the actions

taken by the licensee, this item is closed.

'

IV Plant Support

,

R1

Radiological Protection and Chemistry Controls

1

.

R1.1 General Radiological Controls

'

Insoection Scone (71750)

'

General Health Physics (HP) activities were observed during the

report period.

This included locked high radiation area doors,

proper radiological postings, and personnel frisking upon exiting

the Radiologically Controlled Area (RCA).

The inspectors made

i

Enclosure 2

.

.

.

.

.

-

-

.

,

30

frequent tours of the RCA and discussed radiological controls with

HP technicians and HP management.

No significant deficiencies

'

were identified.

R1.2 Radiological Controls

j

a.

Insoection Scooe (83750)

Radiological controls associated with ongoing operational

activities were reviewed and evaluated.

Controls for both routine

operations and specific non-routine tasks were included in the

review

In particular. housekeeping and cleanliness, area

postin s radioactive waste (radwaste) container labels, and

contro s for high radiation areas were reviewed for adequacy.

Licensee controls for ongoing operations were compared against

documented requirements in applicable sections of Technical

i

Specifications (TSs). Final Safety Analysis Report (FSAR). and

10 CFR Part 20.

The inspectors made frequent tours of the RCAs.

In addition.

specific radiation work permit (RWP) procedural guidance and

selected survey results were reviewed and discussed with

responsible HP staff and supervisors.

Operations and radiological

controls associated with the low-level radioactive waste storage

j

building were observed and evaluated.

Controls for specific tasks

'

performed in accordance with the following RWPs were evaluated in

detail.

e

RWP 197-0005. Remove old obsolete drum capping equipment and

support work, effective January 10. 1997.

e

RWP 097-0017. Process / ship / receive / load out/ transport

radioactive materials and support work including alpha trending

and Waste Separation and Temporary Storage Facility (WSTSF)

work, effective January 10, 1997.

In addition the inspectors reviewed and discussed program

guidance and results of internal exposure evaluations made by the

licensee during 1996.

b.

Observations and Findinas

High and locked high radiation area controls were verified to be

implemented in accordance with TS requirements.

Postings of

radwaste storage areas were proper and in accordance with TS or

10 CFR 20 Subpart J requirements.

Overall, containers holding

radwaste, contaminated materials, and equipment were labeled in

accordance with 10 C.FR 20.1904 requirements.

Excluding activities

associated with construction of a hot tool room and an isolated

example of trash and debris in the Unit 2 (U2) Radioactive Waste

Enclosure 2

--

.

.

.

.-.

.

.

.

'

,

l

31

(RW) building area 164 foot (*) elevation floor, cleanliness and

housekeeping within the RCAs. outside radwaste ]rocessing and

storage areas, and the low-level waste storage Juilding were

acceptable.

Radiation control activities associated with ongoing

radwaste processing, storage and shipping operations were adequate

and conducted in accordance with applicable RWPs and procedures.

During facility tours, the inspectors observed several poor

radiological control practices associated with demolition of a

'

concrete wall located in the Unit 1 (U1) RW area 132' elevation.

Demolition activities were in preparation for construction of a

hot tool room and were performed under RWP 197-0005. Remove Old

Obsolete Drum Capping Equi) ment and Support Work. effective

January 10.197

The wort area was roped-off equipped with a

step-off pad, cad posted as a Contaminated Area. On

!

January 15. 1997, the ins)ectors noted that the demolition

activities generated visi)le and potentially contaminated dust

which subsequently became airborne and also covered the step-off

pad and areas surrounding the posted area.

The only established

engineering control provided was use of a High Efficiency

Particulate Air (HEPA) filtered portable exhaust ventilation

i

system but without an enclosure surrounding the work area. The

most recent quantitative contamination and air sample survey

results conducted on January 11, 1997, verified contamination on

the wall. approximately 1000 to 3000 disintegration per minute per

l

2

100 centimeters square (dpm/100cm ) but did not identify an

airborne hazard.

However, the inspectors noted that no additional

airborne surveys were conducted within the work area and that the

most recent quantitative radiation surveys completed on

January 13. 1997, were in response to unexpectedly elevated

electronic dosimeter readings.

!

Discussions with responsible HP and maintenance personnel

indicated that the tools used for the demolition changed and that

the staff was aware of the increased levels of potentially

contaminated dust outside of the designated area.

Licensee

representatives stated that additional gross contamination surveys

of the floor conducted outside of the posted area using Masslin

cloth were conducted but not documented.

Responsible HP personnel

stated that the gross surveys did not indicate any contamination

outside of the roped-off area. TS 5.4 requires that written

procedures be established implemented, and maintained covering

activities delineated in Appendix A of Regulatory Guide (RG) 1.33.

Rev. 2. dated February 1978.

Regulatory Guide 1.33. Appendix A.

" Typical Procedures for Pressurized Water Reactor and Boiling

Water Reactors." Paragraph 7.e. requires radiation protection

procedures for Radiation Work Permit System and for Contamination

Control.

Health Physics procedure 60AC-HPX-004-0S, Radiation and

Contamination Control. Revision (Rev.) 14. effective October 15,

1996, specifies that HP will:

initiate controls, e.g..

Enclosure 2

L

-

-

-

_ ___ _ _

_

_.

.

.

32

l

engineering controls, to ensure that spread of contamination is

minimized; will perform non-routine radiation and contamination

surveys as required, to support operation and maintenance: will

-

perform airborne su veys during radioactive work which is expected

to cause airborne radioactivity unless constant air monitors are

,

provided: and perform periodic air sampling to evaluate the

effectiveness of filtered ventilation used to control airborne

radioactivity. The inspectors noted that the established

engineering controls and the contamination and airborne surveys

conducted for the observed demolition activities were not in

,

accordance with the established procedure.

]

The inspectors did not identify any significant concerns regarding

use of the whole body counter (WBC) equipment used for in vivo

.

analyses and results.

Excluding concerns identified for WBC

calibration guidance detailed in Paragraph R7.1. the applicable

licensee procedures were determined to be satisfactory and staff

knowledge adequate to implement the current program.

Potential

procedural enhancements discussed with responsible licensee

representatives included:

improved guidance for evaluating

potential internal exposure resulting from non-gamma-emitting

i

radionuclides; collection methods for bioassay sam)les and

associated vendor capabilities; and inclusion of t1e standup WBC,

t

currently used for qualitative (screening) analyses, in the

crosscheck program.

Results of all )ositive internal ex)osures of

workers analyzed in 1996 were less tlan one percent of tie Annual

Limits of Intake (ALIs) documented in 10 CFR Part 20.

'

c.

Conclusions

Radiological controls for high and locked high radiation areas

were maintained in accordance with TS requirements. Area postings

and container radiation labels were appro)riate. Housekeeping and

cleanliness were adequate.

In general, t1e licensee was

controlling internal exposure effectively.

The poor engineering

controls and survey practices observed were identified as an

example of VIO 50-321, 366/96-15-05: Failure to Follow Procedures

for Contamination Control and for Deficiency Card Issuance for

Inadequate Bioassay Calibration Guidance.

R5

Staff Training and Qualifications in Radiation Protection and

Chemistry

a.

Insoection Scone (83750)

General employee training provided to meet the requirements of

10 CFR Part 19. and specific training and medical certification.

required by 10 CFR Part 20 for persons who used or were designated

to wear respiratory protective equipment. were reviewed and

evaluated during the onsite inspection.

Enclosure 2

,

,

33

Selected 1996 training and medical certification records for

selected personnel within the following groups were reviewed and

discussed with responsible licensee representatives.-

Personnel evaluated by the licensee for potential internal

e

exposure during 1996.

e

All licensee and contract personnel involved in the transfer of

a full radwaste liner from the radwaste processing facilities

to a shipping cask during the week of January 13. 1997.

e

All contract personnel involved with routine operations at the

low-level radioactive waste storage building.

b.

Observations and Findinas

The inspectors verified that general employee and respiratory

protection training, and medical certifications were conducted in

accordance with training procedure 73TR-T-RN-001-0S General

Employee Training Programs. Rev. 9. effective June 1. 1996.

The

guidance met the requirements of 10 CFR 19.13 and 10 CFR 20.1703.

Review and discussion of training records verified that all

)ersonnel met the required general employee training requirements.

rom review of training records and selected Respirator Device

Issuance Reports, the inspectors verified that all persons who

used respiratory protection equipment were trained and medically

certified in accordance with the applicable procedures.

c.

Conclusions

General employee training and completed medical certifications for

personnel involved in licensed activities were conducted in

accordance with the a)plicable procedures and met the applicable

requirements of 10 CFR 19 and 10 CFR 20.

R7

Quality Assurance in Radiation Protection and Chemistry Activities

R7.1

In Vivo Ouality Control Analyses

a.

Insoection Scooe (83750. 84750)

During the inspection, the 1996 quarterly Quality Control (OC)

cross-check results for the in vivo WBC quantitative (chair

geometry) radionuclide analyses were reviewed and discussed.

b.

Observations and Findinos

For the first and fourth quarter cross-check samples, all results

for torso, lung and thyroid were in agreement with the vendor

Enclosure 2

j

-..

_

._

._

_ _ . _ _ _

._._. .

. _ _

.

__.

_.

!

l

.

.

i

!

34

!

i

values.

Disagreements between selected licensee analysis results

i

and the known values were identified for the second and third

cuarters of 1996. -For the second quarter samples analyzed on

!

Fay 23, 1996, the identified disagreements resulted from an

<

improper calibration conducted April 23, 1996.

Responsible

i

licensee representatives stated that the improper calibration

,

resulted from misinterpretation of calibration guidance provided

l

by the vendor software-driven calibration menu.

.

!

From review of the applicable procedure and discus. ions with

cognizant licensee representatives, the inspectors determined that

i

no changes to, nor 3rocedural warnings regarding applicable

i

computer-based cali] ration menu were implemerted.

A licensee

review of.the WBC chair in vivo analysis results determined that

the improper calibration had no significant effect on assignment

l

of internal exposure for the two individuals who were evaluated

i

using the WBC chair between the dates of the improper calibration

l

and when the deficiency was identified and corrected. However,

the inspectors noted that the subject evaluations were not

documented.

The inspectors noted that RG 1.33 recommends written

procedures for bioassay programs and that contrary to

,

administrative control procedure 10AC-MGR-004-05. Deficiency

l

Control System, Rev.10. dated March 3,1996, a Deficiency Card

i

for the calibration procedural inadequacy was not initiated.

For

the third quarter, disagreements in results of the crosscheck

comparisons resulted from failure to load all the provided cross-

i

check samples and did not affect the calibration accuracy.

1

'

c.

Conclusions

Quality control cross-check analyses were conducted in accordance

with procedural requirements.

However, the failure to issue a

deficiency card was identified as an additional example of

.

procedural VIO 50-321, 366/96-15-05: Failure to Follow Procedures

for Issuance of a Deficiency Card for Inadequate Bioassay

Calibration Procedural Guidance.

'

{

R8

Miscellaneous Radiation Protection and Chemistry Issues

l

a.

Insoection Scooe (83750. 84750. 86750)

I

The status of selected radiation control and radwaste performance

indicators was reviewed and discussed with licensee

,

j

representatives.

i'

b.

Observations and Findinas

i'

Since 1993, annual dose expenditure per unit outage continued to

decrease.

For 1996, dose expenditure was approximately 441

person-rem and was within the established goal of 575 person-rem.

Enclosure 2

,

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-

-

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.

.r.

,

,,.,-.r

,

.-

-v--

, .

-

- - - - - - -

. . -

-

.

-

-

_ .

-

-

_-- . _

_ - . _ - . -

. - - - - -

.- _

.-

<

i

35

For 1996, licensee representatives informed the inspectors that no

I

abnormal effluent releases were identified.

The 1996 dose

!

estimates from both liquid and gaseous effluents were small

l

percentages of the Offsite Dose Calculation Manual (ODCM) limits.

l

No significant trends or changes in radiological environmental

i

monitoring program sample radiological analyses were identified.

l

!

c.

Conclusions

j

Radiation protection performance indicators verified that licensee

actions to control worker dose were effective and radiological

effluent releases were minimized.

j

R8.1

(Closed) Insoector Followuo Item (IFI) 50-321. 366/95-05-01:

-

Review Post Accident Samolina System (PASS) Proaram Enhancements.

[

This item was opened pending completion of equipment modifications

and procedural changes identified for the PASS system by the

!

licensee.

From selected comparison of installed PASS equipment

,

j

with configuration control documents arid review of current

procedures, the inspectors verified completion of modifications

,

and procedural revisions.

On January 16, 1997, the inspectors

observed licensee representatives successfully demonstrate PASS

operability by collecting, processing, and analyzing a U2 reactor

coolant system (RCS) liquid sample in accordance with Chemistry

(CH) Sampling (SAM) procedure 64CH-SAM-020-0S, Rev. 1.

From

review of selected August 1996 through January 1997 PASS In-Line

Analyses records and discussions with the licensee, the ins)ectors

verified that both containment air and RCS samples from bot 1 U1

and U2 were collected and processed by chemistry personnel using

the PASS equipment on a routine basis.

Excluding several

instances of low RCS pH determinations relative to reference

samples, no other analysis accuracy issues were identified. The

licensee stated that a review of the low pH values would be

conducted. As of November 1996. PASS availability was listed as

95 percent in licensee maintenance records.

Based on licensee

actions and current system reliability. this item is closed.

R8.2

(Closed) Unresolved Item (URI) 50-321. 366/96-14-07:

Determine if

Certificate of Comoliance (C0C) and Associated Vendor Documents

for Packaae No. USA /5805/B() Were Controlled in Accordance with

Administrative Procedure 20AC-ADM-003-05. Vendor Manual Review and

Control.

During review of C0Cs and associated documentation for package

type USA /5805/B() used for an August 7, 1996 Type B shipment of

irradiated hardware to a licensed burial facility, the inspectors

determined that current manuals and procedures were received

directly by the radaaste staff from the vendor. However, the

inspectors noted that the subject documents may not have been

Enclosure 2

..-

.- - -

-

.

.

--

.

---

.

. -

.-

-

.

-

- .

-

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,

36

i

reviewed and controlled in accordance with the applicable

administrative procedure, and thus may not have met the intent of

i

10 CFR 70.113 quality assurance (0A) requirements for shipping

program activities. A review of licensee records identified that

the C0C and procedures were maintained in accordance with the

applicable administrative procedure. However, the licensee was

unable to demonstrate that the subject manual was received.

!

reviewed, processed, and maintained in accordance with the subject

administrative control procedure. All other documents associated

with shi) ping containers which were, or could be used to make

,

Type B slipments were maintained in accordance with the licensee *s

procedure.

1

Prior to the current inspection. the licensee requested all

uncontrolled copies of C0Cs. and associated documents from staff

members involved in transportation activities.

The inspectors

reviewed a January 7.1997, letter confirming that a single copy

of shipping container documents would be sent to the licensee.

Consistent with Section IV of the Enforcement Policy based on

!

corrective actions taken prior to the end of the inspection, this

i

issue was identified as Non-cited Violation (NCV)

t

50-321, 366/96-15-06: Failure to Maintain Shipping Cask Manuals in

Accordance with Established Procedures to Meet 10 CFR Part 70.113.

52

Status of Security Facilities and Equipment

!

The inspectors toured the protected area and observed that the

perimeter fence was intact and not compromised by erosion nor

i

disrepair. The fence fabric was secured and barbed wire was

i

angled as required by the licensee's Plant Security Program (PSP).

Isolation zones were maintained on both sides of the barrier and

were free of objects which could shield or conceal an individual.

!

The inspectors observed personnel and packages entering the

protected area were searched either by special purpose detectors

or by a physical patdown for firearms, explosives and contraband.

Badge issuance was observed, as was the processing and escorting

,

of visitors.

Vehicles were searched, escorted and secured as

described in the PSP.

)

The inspectors concluded that the areas of the PSP inspected met

the PSP requirements.

V. Manaaement Meetinos

,

X.

Review of UFSAR Commitments

A recent discovery of a licensee operating its facility in a

i

manner contrary to the Updated Final Safety Analysis Report

(UFSAR) description highlighted the need for a special focused

review that compares plant practices, procedures and/or parameters

Enclosure 2

l

l

-

.

.

.

'

k

e,

37

to the UFSAR description. While performing the ins)ections

discussed in this re) ort, the inspectors reviewed t1e applicable

portions of the UFSAR that related to the areas inspected. The

inspectors verified that the UFSAR wording was consistent with the

observed plant practices procedures, and/or parameters.

X.1

Exit Meeting Summary

The inspectors presented the inspection results to members of the

licensee management-at the conclusion of the inspection on

January 31, 1997.

The licensee acknowledged the findings

presented. An interim exit was conducted on January 17, 1997.

The inspectors asked the licensee whether any materials examined

during the inspection should be considered proprietary.

No

proprietary information was identified.

X.2

Refueling Outage Management Meeting

The inspectors attended several Outage Management Meetings

conducted at the site. Among the items discussed were: The

Fall 1997. Unit 1 outage status: the Spring 1997. Unit 2 outage

status: the Unit 2 maintenance planning update: the Unit 2 scope

additions: the status of outage requisitions; and the status of

design changes. The ins ectors observed that the critical path

was identified as the hi h pressure turbine modifications. A fuel

shuffle, and not a fuel

ff load, will be performed.

However. the

'

visual inspection of the vessel internal core spray piping could

>

impact the outage schedule.

The inspectors concluded that the

'

outage is well planned. with realistic goals, with adequate

.

support.

!

X.3

Management Meeting in Region II Office

i

i

A licensee-requested meeting was held in the Nuclear Regulatory

Commission (NRC) office in Atlanta. Georgia on January 8.1997.

.

The purpose of the meeting was to discuss Georgia Power Company's

!

Self-Assessment for the Hatch nuclear plant.

The NRC concluded

that the meeting was beneficial in that it provided a better

>

t

understanding of accomplishments and improvement initiatives at

the Hatch facility.

A meeting summary was documented under

l

separate correspondence dated January 9. 1997.

.

4

Enclosure 2

- --

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i

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, ..

38

1

,

\\

PARTIAL LIST OF PERSONS CONTACTED

)

Licensee

Anderson, J., Unit Superintendent

Betsill, J., Operations Manager

!

Coggin

C., Engineering Support Manager

i

Curtis, S., Operations Support Superintendent

!

Davis

D., Plant Administration Manager

!

Fornel, P., Performance Team Manager

Fraser, 0., Safety Audit and Engineering Review Supervisor

Hammonds, J., Regulatory Compliance Supervisor

Kirkley, W., Health Physics and Chemistry Manager

Lewis, J., Training and Emergency Preparedness Manager

Moore, C,. Assistant General Manager - Plant Support

Reddick, R., Site Emergency Preparedness Coordinator

Roberts, P., Outages and Planning Manager

Sumner, H., General Manager - Nuclear Plant

!

Thompson, J., Nuclear Security Manager

Tipps, S., Nuclear Safety and Compliance Manager

>

,

Wells, P., Assistant General Manager - Operations

l

!

INSPECTION PROCEDURES USED

'

-

IP

'551: Onsite Engineering

IP 90500:

Effectiveness of Licensee Controls in

-

Identifying, Resolving, and Preventing Problems

l

IP 61726:

Surveillance Observations

IP 62700: Maintenance Implementation

IP 62703:

Maintenance Observations

IP 62707: Maintenance Observations

IP 71707:

Plant Operations

IP 71714: Cold Weather Preparations

IP 71750:

Plant Support Activities

IP 83750: Occupational Radiation Exposure

IP 84750:

Radioactive Waste Treatment and Effluent and

Environmental Monitoring

IP 86750: Solid Radioactive Waste Management and

Transportation of Radioactive Materials

IP 92700: Onsite Follow-up of Written Reports of Nonroutine

Events at Power Reactor Facilities

IP 92901:

Followup - Operations

IP 92902:

Followup - Maintenance / Surveillance

IP 92903:

Followup - Followup Engineering

IP 92904:

Followup - Plant Support

j

Enclosure 2

I

.

.

.

_

. .

-

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_7

_ . _

_

_

_ _ _ _ .

_ . _ _ _ _ _ . _ _ _ _ _ . _ _

_.

. - _ _

,

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!

39

i

ITEMS OPENED. CLOSED. AND DISCUSSED

'

Ooened

j

50-366/96-15-01

NCV Inadequate Procedures for Replacement of the

Unit 2 Drywell Hydrogen Recombiner Flow

Controller Batteries and Establishing the

j

Required Controller " Dead Band" Following

Certain Maintenance Activities identified

(Section M2.1).

j

50-321/96-15-02

VIO Maintenance Personnel Failure To Follow

Procedure During Valve backseating Activities

i

(Section M3.2).

'

50-321.366/96-15-03 IFI Resolution of RCIC and HPC1 Turbine Speed

Control Drift Units 1 and 2. respectively

(Section M3.3).

50-321.366/96-15-04 IFI Switchyard Maintenance and Material Condition

(Section M1.4).

50-321.366/96-15-05 VIO Failure to Follow Procedures for Contamination

Control and for Deficiency Card Issuance for

Inadequate Bioassay Calibration Guidance

(Sections R1.2 and R7.1).

l

50-321.366/96-15-06 NCV Failure to Maintain Ship)ing Cask Manuals in

accordance with Establisled Procedures to Meet

'

10 CFR Part 70.113 (Section R8.2).

!

Closed

50-366/96-15-01

NCV Inadequate Procedures for Repl6 cement of the

Unit 2 Drywell Hydrogen Recombiner Flow

,

Controller Batteries and Establishing the

,

Required Controller " Dead Band" Following

Certain Maintenance Activities (Section M2.1).

50-321.366/96-15-06 NCV Failure to Maintain Ship)ing Cask Manuals in

Accordance with Establisled Procedures to Meet

10 CFR Part 70.113 (Section R8.2).

50-321.366/96-14-07 URI Deteimine if Certificate of Compliance (C0C) and

Associated Vendor Documents for Package

No. USA /5805/B() Were Controlled in Accordance

with Administrative Procedure 20AC-ADM-003-0S.

Vendor Manual Review and Control (Section R8.2).

Enclosure 2

.

.

. ..

40

50-321/96-14

LER Incorrect Circuit Breaker Setting

Results in Emergency Diesel Generator Being

Inoperable (Section EB.1).

50-321/96-14. R1

LER Incorrect Circuit Breaker Setting

Results in Emergency Diesel Gcnerator Being

Inoperable (Section E8.2).

50-321.366/96-08 LER Inadequate Procedure Results in Reactor Pressure

Increate and Automatic Reactor Scram

(Section E8.5).

50-321/96-07

LER Failed Com)onent Results in Inadvertent

Emergency )iesel Generator Start (Section E8.4).

50-321/96-07-03

IFI Degradation and Replacement of Unit 2 Station

Service Battery 2B Due to Buildup of Cell

Sediment (Section E8.3).

50-321/96-06

LER Inadequate Procedure and Lack of Work

Coordination Result in Withdrawal of Inoperable

!

Control Rod (Section M8.2).

50-321.366/95-05-01 IFI Review Post Accident Sampling System (PASS)

Program Enhancements (Section R8.1).

S0-321/96-06-04

VIO Failure to Meet TS Surveillance Requirements

Prior to Withdrawal of a Control Rod While in

Cold Shutdown (Section M8.1).

Enclosure 2

--

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,

41

LIST OF ACRONYMS USED

l

l

ALARA- As Low as Reasonably Achievable

Annual Limit of Intake

ALI

i

-

ANSI - American National Standards Institute

i

Building and Grounds

l

B&G

-

BOST - Beginning Of Shift Training

CFR - Code of Federal Regulations

AGM-PS- Assistant General Manager, Plant Support

1

CH

- Chemistry

cm

- centimeter

l

C0C - Certificate of Compliance

Control Room

CR

-

degrees Fahrenheit

j

  • F

-

Deficiency Card

DC

t

-

DG

- Diesel Generator

disintegrations per minute

dpm

-

ECCS - Emergency Core Cooling Systems

i

EDG - Emergency Diesel Generator

!

Electronic Governor Motor

i

EGM

-

Electro Hydraulic Control

EHC

-

FME - Foreign Material Exclusion

FSAR - Final Safety Analysis Report

Georgia Power Company

GPC

-

HEPA - High-Efficiency Particulate Air Filters

Hatch Nuclear Plant

HNP

-

HP

- Health Physics

HPCI - High Pressure Coolant Irjection

HRS - Hydrogen Recombiner System

Instrument and Control

I&C

-

IFI

-

Inspector Followup Item

IR

-

Inspection Report

IST

Inservice Testing

-

Kilowatt

KW

-

KVAR - Kilovolts Ampere Reactive

LER - Licensee Event Report

LPCI - Low Pressure Coolant Injection

MCC - Motor Control Center

MG

- Motor Generator

MOV - Motor Operated Valve

MWO - Maintenance Work Order

Non-Cited Violation

NCV

-

NRC - Nuclear Regulatory Commission

NRR - Nuclear Reactor Regulation

,

i

NS&C - Nuclear Safety and Compliance

,

ODCM - Offsite Dose Calculation Manual

l

i

PASS - Post Accident Sample System

PDR

Public Document Room

-

Plant Equipment Operator

PE0

-

,

PM

- Preventative Maintenance

.

Enclosure 2

l

,

h-

-

-

. -

- - ..

. - - . -

_ , , . - , _ _ . _ - . - - _ - _ . _ , _ _

t

"

..

3

42

PSIG -

Pounds Per Square Inch Gauge

PSP - Plant Security Program

PSW - Plant Service Water System

OA

- Quality Assurance

QC

- Quality Control

RCA - Radiologic 61 Controlled Area

RCS - Reactor Coolant System

RCIC - Reactor Core Isolation Cooling

Rev - Revision

RG

- Regulatory Guide

RHR - Residual Heat Removal

RHRSW- Residual Heat Removal Service Water

RPM - Revolutions Per Minute

RPS - Reactor Protection System

RR

- Reactor Recirculation

RTP -

Rated Thermal Power

RW

- Radioactive Waste

RWCU - Reactor Water Clean-up

RWP - Radiation Work Permit

SAM - Sampling

SCBA - Self Contained Breathing Apparatus

SCFM - Standard Cubic Feed Per Minute

SLC - Ltandby Liquid Control

SRM - Source Range Monitor

SRV - Safety Relief Valve

SSB - Station Service Battery

TRAQS- Training Record and Qualification System

TRM - Technical Requirements Manual

TS

- Technical Specifications

Ul.U2- Unit 1. Unit 2

UFSAR- Updated Final Safety Analysis Report

URI

- Unresolved Item

VAC - Volts Alternating Current

VIO - Violation

WBC - Whole Body Counter

WSTSF- Waste Separation and Temporary Storage Facility

,

Enclosure 2