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!                               U.S. NUCLEAR REGULATORY COMMISSION
!
                                              REGION II
U.S. NUCLEAR REGULATORY COMMISSION
          Docket Nos:     50-413, 50-414
REGION II
          License Nos:     NPF-35 NPF-52
Docket Nos:
          Report Nos.:     50-413/97-07. 50-414/97-07
50-413, 50-414
License Nos:
NPF-35 NPF-52
Report Nos.:
50-413/97-07. 50-414/97-07
i
Licensee:
Duke Power Company
Facility:
Catawba Nuclear Station Units 1 and 2
Location.
422 South Church Street
Charlotte. NC 28242
Dates:
March 23 - April 26,1997
Inspectors:
R. J. Freudenberger, Senior Resident Inspector
P. A. Balmain, Resident Inspector
R. L. Franovich. Resident Inspector
R. A. Gibbs, Resident Inspector (In Training)
.
J. L. Coley, Jr. . Reactor Inspector (Sections M2, E2.1)
D. B. Forbes, Radiation Specialist (Sections R1, R5, R7)
W. H. Miller, Jr.. Reactor Inspector (Sections 08.1, F2,
F3. FS, F6. F7 F8)
R. L. Moore, Reactor Inspector (Sections E2.2, E4.1, E8.1.
E8.2)
Approved by:
C. A. Casto, Chief
Reactor Projects Branch 1
Division of Reactor Projects
i
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          Licensee:        Duke Power Company
          Facility:        Catawba Nuclear Station Units 1 and 2
          Location.        422 South Church Street
                          Charlotte. NC 28242
          Dates:          March 23 - April 26,1997
          Inspectors:      R. J. Freudenberger, Senior Resident Inspector
                          P. A. Balmain, Resident Inspector
                          R. L. Franovich. Resident Inspector
  .
                          R. A. Gibbs, Resident Inspector (In Training)
                          J. L. Coley, Jr. . Reactor Inspector (Sections M2, E2.1)
                          D. B. Forbes, Radiation Specialist (Sections R1, R5, R7)
                          W. H. Miller, Jr.. Reactor Inspector (Sections 08.1, F2,
                              F3. FS, F6. F7 F8)
                          R. L. Moore, Reactor Inspector (Sections E2.2, E4.1, E8.1.
                              E8.2)
          Approved by:    C. A. Casto, Chief
                          Reactor Projects Branch 1
                          Division of Reactor Projects
                                                                                        i
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!
!
                                                                            Enclosure 2
Enclosure 2
      9706050102 970523
9706050102 970523
      PDR   ADOCK 05000413
PDR
      G               PDR       :
ADOCK 05000413
G
PDR
:


                                                                                      !
!
      '
'
    .
.
                                        EXECUTIVE SUMMARY
EXECUTIVE SUMMARY
                              Catawba Nucleer Station. Units 1 & 2                     4
Catawba Nucleer Station. Units 1 & 2
                        NRC Inspection Report 50-413/97-07. 50-414/97-07               '
4
        This integrated inspection included aspects of licensee operations.             !
NRC Inspection Report 50-413/97-07. 50-414/97-07
        maintenance, engineering, and plant support. The report covers a 6-week
'
        period of resident ins)ection: in addition. it includes the results of
This integrated inspection included aspects of licensee operations.
        announced inspections ay regional reactor safety inspectors.                   l
maintenance, engineering, and plant support. The report covers a 6-week
        Operations
period of resident ins)ection: in addition. it includes the results of
        .    A Unit 2 loss of spent fuel pool cooling, which was caused by an
announced inspections ay regional reactor safety inspectors.
              inadequate containment penetration test procedure, was identified as a
Operations
              violation. Other barriers that could have prevented the event included   l
A Unit 2 loss of spent fuel pool cooling, which was caused by an
              increased emphasis on the importance of the system function during the   l
.
              pre-job brief and more diligent control board monitoring. The
inadequate containment penetration test procedure, was identified as a
              operator's performance in response to the event was appropriate. The     l
violation.
              Catawba Safety Review Group evaluation of the event was detailed and     I
Other barriers that could have prevented the event included
              identified substantive corrective actions. (Section 01.1)
increased emphasis on the importance of the system function during the
        *    Midloop Activities were well controlled. Nevertheless, the process for
l
              restoring equipment necessary for gravity flows to the core may not be
pre-job brief and more diligent control board monitoring.
              ensured by administrative controls. (Section 01.2)
The
  .
operator's performance in response to the event was appropriate.
        .    The inspector concluded that selected initial conditions for the
The
              compensatory action associated with the main control room pressure       i
Catawba Safety Review Group evaluation of the event was detailed and
              boundary were satisfied. The inspector further concluded that operator
identified substantive corrective actions. (Section 01.1)
              effectiveness in im)lementing this complex compensatory action was       I
Midloop Activities were well controlled.
              challenged by lengtly initial conditions, and the practice of not         '
Nevertheless, the process for
              periodically reverifying required initial conditions. (Section 01.3)
*
                                                                                        i
restoring equipment necessary for gravity flows to the core may not be
        .    Problems encountered with the Boron Dilution Mitigation System during
ensured by administrative controls. (Section 01.2)
              the Unit 2 refueling outage were indicative of historically low
.
              reliability and availability, which caused additional control room
The inspector concluded that selected initial conditions for the
              operator workload to compensate for the system's low reliability.
.
              (Section 01.4)
compensatory action associated with the main control room pressure
        .    The inspector concluded that actions by operations and Radiation
i
              Protection personnel in response to the radiation alarm in the fuel
boundary were satisfied.
              handling building were good. However. foreign material exclusion
The inspector further concluded that operator
effectiveness in im)lementing this complex compensatory action was
challenged by lengtly initial conditions, and the practice of not
'
periodically reverifying required initial conditions. (Section 01.3)
i
Problems encountered with the Boron Dilution Mitigation System during
.
the Unit 2 refueling outage were indicative of historically low
reliability and availability, which caused additional control room
operator workload to compensate for the system's low reliability.
(Section 01.4)
The inspector concluded that actions by operations and Radiation
.
Protection personnel in response to the radiation alarm in the fuel
handling building were good. However. foreign material exclusion
administrative controls were not properly im)lemented by personnel
'
'
              administrative controls were not properly im)lemented by personnel
working in the fuel transfer canal area of t1e fuel handling building.
              working in the fuel transfer canal area of t1e fuel handling building.
(Section 01.5)
              (Section 01.5)
!
!
        .    A Unit 1 pressurizer )ower operated relief block valve control circuit
A Unit 1 pressurizer )ower operated relief block valve control circuit
              failure occurred whic1 is a potential repeat of a previous 1995 failure.
.
              The licensee has planned appropriate actions to determine the cause of
failure occurred whic1 is a potential repeat of a previous 1995 failure.
              the control circuit component failure. (Section 01.6)
The licensee has planned appropriate actions to determine the cause of
                                                                      Enclosure 2
the control circuit component failure. (Section 01.6)
Enclosure 2
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                                                .   _       _   _
.
        '
_
      .
_
                .
_
                                                  2
'
          Maintenance
.
          .    The inspector concluded that, in general, outage-related maintenance
.
                activities were ap]ropriately conducted. Although multiple barriers to
2
                minimizing the risc of human error during reactor coolant pump seal
Maintenance
                maintenance were noted, the inspector was unaware of any human
The inspector concluded that, in general, outage-related maintenance
                performance problems associated with the work. (Section M1.1)
.
          .    The licensee's resolution of long-standing elevated vibration levels
activities were ap]ropriately conducted. Although multiple barriers to
                associated with the Unit 2B nuclear service water pump motor was very
minimizing the risc of human error during reactor coolant pump seal
                good.   Deficiencies identified with a spare nuclear service water pump
maintenance were noted, the inspector was unaware of any human
                motor, a previous motor failure, and findings identified by licensee
performance problems associated with the work. (Section M1.1)
                assessments of warehouse storage and handling practices raised questions
The licensee's resolution of long-standing elevated vibration levels
                about control and storage of spare motors. The issue is identified as
.
                an Inspector Followup Item and will be reviewed during a future
associated with the Unit 2B nuclear service water pump motor was very
                inspection. (Section M1.2)
good.
          *    Certification records for nondestructive examination (NDE) personnel,
Deficiencies identified with a spare nuclear service water pump
                weld examinations, and NDE examination procedures were in accordance
motor, a previous motor failure, and findings identified by licensee
                with Code requirements. (Section M2.1)
assessments of warehouse storage and handling practices raised questions
  .      *    Review of the eddy current outage plan, equipment setup and acquisition
about control and storage of spare motors. The issue is identified as
                procedures, personnel and equipment certifications, and observation of
an Inspector Followup Item and will be reviewed during a future
                data acquisition activities revealed that required documentation was
inspection. (Section M1.2)
                available and complete, and data acquisition personnel were
Certification records for nondestructive examination (NDE) personnel,
    -
*
                knowledgeable of the eddy current examination process. (Section M2.2)
weld examinations, and NDE examination procedures were in accordance
          +    The licensee has implemented an effective program for the detection of
with Code requirements. (Section M2.1)
                flow accelerated corrosion in components. This program is based on
Review of the eddy current outage plan, equipment setup and acquisition
                recommendations found in recognized industry standards. (Section M2.3)
*
          .    The maintenance / work control self-assessment programs effectively
.
                identified areas for improvement and a]propriate corrective actions.
procedures, personnel and equipment certifications, and observation of
                The self-assessments apparently contri)uted to improvement in the
data acquisition activities revealed that required documentation was
                performance of the Maintenance and Work Control organizations. (Section
available and complete, and data acquisition personnel were
                M7.1)
-
          Enaineerina
knowledgeable of the eddy current examination process. (Section M2.2)
          .    The licensee's actions to replace all control rod assemblies that had
The licensee has implemented an effective program for the detection of
                evidence of tip cracking were appropriate. (Section El.1)
+
          *    Documentation for the modification of the Unit 2 pressurizer manway was
flow accelerated corrosion in components. This program is based on
                satisfactory, and engineering considerations for the modification,
recommendations found in recognized industry standards. (Section M2.3)
                inspection, and cleaning of the pressurizer were very good. (Section
The maintenance / work control self-assessment programs effectively
                E2.1)
.
          *    Design controls for Unit 2 outage modifications were consistent with
identified areas for improvement and a]propriate corrective actions.
                regulatory requirements. (Section E2.2)
The self-assessments apparently contri)uted to improvement in the
                                                                        Enclosure 2
performance of the Maintenance and Work Control organizations. (Section
M7.1)
Enaineerina
The licensee's actions to replace all control rod assemblies that had
.
evidence of tip cracking were appropriate. (Section El.1)
Documentation for the modification of the Unit 2 pressurizer manway was
*
satisfactory, and engineering considerations for the modification,
inspection, and cleaning of the pressurizer were very good. (Section
E2.1)
Design controls for Unit 2 outage modifications were consistent with
*
regulatory requirements. (Section E2.2)
Enclosure 2
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  .- . -- - - - . . _ - - - - . ~                                             - - - . - - -                       - . - . . .
.- . -- - - - . . _ - - - - . ~
- - - . - - -
- . - . . .
t
t
                        ,
,
          *
*
                              ,                                                                                               ;
,
                                                                                                                              .
;
                                          .
.
                                                                                                                              .
.
.
'
'
                                                                            3
3
                                                                                                                              ,
,
                                                                                                                              '
The motor shaft key way cracking in large high speed limitorque motor
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                                  .     The motor shaft key way cracking in large high speed limitorque motor
'
                                        actuators at-Catawba was an example of good identification and                         ;
.
actuators at-Catawba was an example of good identification and
;
resolution of equipment problems using the Operating Experience Program.
'
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'
'
                                        resolution of equipment problems using the Operating Experience Program.              '
(Section E4.1)
                                        (Section E4.1)
L
L                                 Plant Sucoort
Plant Sucoort
                                  .    The licensee was effectively maintaining controls for personnel                       .
The licensee was effectively maintaining controls for personnel
                                        monitoring, control of radioactive material, radiological postings. and               J
.
                                        radiation area /high radiation area controls as required by 10 CFR Part                 i
.
                                        20. One Non-Cited Violation was identified for failure to source check
monitoring, control of radioactive material, radiological postings. and
                                                                                                                                '
J
l                                       survey instruments as required by licensee procedure. (Section R1.1)
radiation area /high radiation area controls as required by 10 CFR Part
[                                .    The licensee was maintaining programs for controlling exposures As Low                   I
20. One Non-Cited Violation was identified for failure to source check
              '
'
                                        As Reasonably Achievable and continued to be effective in controlling                     '
l
l                                       overall collective dose. (Section R1.2)
survey instruments as required by licensee procedure. (Section R1.1)
                                  .    Radiation protection technicians and radiation workers were receiving an
The licensee was maintaining programs for controlling exposures As Low
[
.
As Reasonably Achievable and continued to be effective in controlling
'
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overall collective dose. (Section R1.2)
Radiation protection technicians and radiation workers were receiving an
.
appropriate level of training to perform work activities involving
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                                        appropriate level of training to perform work activities involving                      )
radiation and/or radioactive material. (Section RS)
                                        radiation and/or radioactive material. (Section RS)
L
L                                 .    The licensee was performing Quality Assurance Audits and effectively
The licensee was performing Quality Assurance Audits and effectively
:.                                     assessing the radiation protection program as required by 10 CFR Part
.
                                        20.1101 and completing corrective actions in a timely manner. (Section
assessing the radiation protection program as required by 10 CFR Part
l                                       R7)
:.
l.                               .    The low number of open maintenance work orders and degraded fire
20.1101 and completing corrective actions in a timely manner. (Section
                                        protection components, in conjunction with the good material condition
l
R7)
l.
The low number of open maintenance work orders and degraded fire
.
protection components, in conjunction with the good material condition
i
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                                        of the fire protection components and fire brigade equipment, indicated
of the fire protection components and fire brigade equipment, indicated
;                                      that, in general     appropriate em3hasis had been placed on the
that, in general
l                                       maintenance and operability of t1e fire protection equipment and
appropriate em3hasis had been placed on the
;
l
maintenance and operability of t1e fire protection equipment and
components. (Section F2.1)
!
'
The work to repair the suction screens for the fire pumps' suction
. -
piping had been ooen since 1991 and was not complete.
The failure to.
complete this work in a timely manner was identified as a Violation.
(Section F2.1)
Good surveillance and test procedures were provided for the fire
.
protection systems and features with effective procedure implementation.
.The coordination of the fire protection water piping cleaning project
was excellent. (Section F2.2)
The fire protection program implementing procedures were good and met
!
!
                                        components. (Section F2.1)
.
licensee and NRC requirements.
Implementation of procedures for the
i
control of. ignition sources, transient combustibles, and general
'
housekeeping was good. An issue regarding time limits for restoration
;
of inoperable fire protection components will be reviewed further by the
'
'
                                  .-    The work to repair the suction screens for the fire pumps' suction
.
                                        piping had been ooen since 1991 and was not complete. The failure to.
l
                                        complete this work in a timely manner was identified as a Violation.
NRC under an Inspector Followup Item.
                                        (Section F2.1)
(Section F3)
                                  .    Good surveillance and test procedures were provided for the fire
4
                                        protection systems and features with effective procedure implementation.
                                      .The coordination of the fire protection water piping cleaning project
                                        was excellent. (Section F2.2)
!                                .    The fire protection program implementing procedures were good and met
                                        licensee and NRC requirements. Implementation of procedures for the                    i'
                                        control of. ignition sources, transient combustibles, and general
                                        housekeeping was good. An issue regarding time limits for restoration                  ;
.                                      of inoperable fire protection components will be reviewed further by the                '
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                                        NRC under an Inspector Followup Item.               (Section F3)
:
:
                                                                                                        Enclosure 2
Enclosure 2
'
'
            - -       -       - --       . - , . . ._     -.         -             .           .   .-
- -
-
- --
. - , . .
._
-.
-
.
.
.-
.
. .-.


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          -
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!                                            4
!
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The fire brigade organization and training met the requirements of the
.
'
'
        .
site procedures.
          The fire brigade organization and training met the requirements of the
Performance by the fire brigade during a drill was
          site procedures. Performance by the fire brigade during a drill was
excellent. The use of the fire brigade safety officer position used
          excellent. The use of the fire brigade safety officer position used
during fire emergencies was identified as a program strength. (Section
          during fire emergencies was identified as a program strength. (Section
F5)
          F5)
l
l       .
Strong coordination and oversight were provided over the facility's fire
          Strong coordination and oversight were provided over the facility's fire
.
          protection program. The Fire Protection BEST was a positive force in
protection program.
          the identification of potential problems and in the development and
The Fire Protection BEST was a positive force in
l         implementation of enhancements to the fire protection program. (Section
the identification of potential problems and in the development and
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implementation of enhancements to the fire protection program. (Section
F6)
,
,
          F6)
!
!
        .
The 1995 audit and assessment of the facility's fire protection program
          The 1995 audit and assessment of the facility's fire protection program
.
          was comprehensive and appropriate corrective action was promptly taken
was comprehensive and appropriate corrective action was promptly taken
          to reso:ve the identified issues. An issue regarding the control of OA
to reso:ve the identified issues. An issue regarding the control of OA
          audit frequencies was identified as an Inspector Followup Item will be
audit frequencies was identified as an Inspector Followup Item will be
          reviewed further by the NRC. (Section F7)
reviewed further by the NRC. (Section F7)
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                                                                  Enclosure 2
Enclosure 2
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                .
.
                                            Report Details
Report Details
        Summary of Plant Status
Summary of Plant Status
        Unit 1 began the ]eriod operating at 100% power and operated at essentially
Unit 1 began the ]eriod operating at 100% power and operated at essentially
        full power througacut the inspection period.
full power througacut the inspection period.
        Unit 2 began the period in cold shutdown (Mode 5) in preparation for the End
Unit 2 began the period in cold shutdown (Mode 5) in preparation for the End
        of Cycle (EOC8) refueling outage. One scheduled period of reactor coolant
of Cycle (EOC8) refueling outage. One scheduled period of reactor coolant
        system reduced inventory /midloop began and completed on April 23.   Midloop was
system reduced inventory /midloop began and completed on April 23.
        entered to support the reactor coolant system vacuum refill evolution. At the
Midloop was
        close of the inspection period the Unit had returned to cold shutdown (Mode 5)   !
entered to support the reactor coolant system vacuum refill evolution. At the
        and heatup activities in preparation for unit restart were beginning.
close of the inspection period the Unit had returned to cold shutdown (Mode 5)
        Review of Uodated Final Safety Analysis Reoort (UFSAR) Commitgents
and heatup activities in preparation for unit restart were beginning.
        While performing inspections discussed in this report, the inspectors reviewed
Review of Uodated Final Safety Analysis Reoort (UFSAR) Commitgents
        the applicable portions of the UFSAR that were related to the areas inspected.   l
While performing inspections discussed in this report, the inspectors reviewed
        The inspectors verified that the UFSAR wording was consistent with the           i
the applicable portions of the UFSAR that were related to the areas inspected.
        observed plant practices, procedures, and/or parameters,                         i
The inspectors verified that the UFSAR wording was consistent with the
                                            I. Operations
i
        01     Conduct of Operations
observed plant practices, procedures, and/or parameters,
  -
i
                                                                                          i
I. Operations
        01.1 Loss of Spent Fuel Pool Coolina
01
            a. Insoection Scope (71707)
Conduct of Operations
                On April 8. Unit 2 was in a refueling outage with all of the fuel off-
i
                loaded to the spent fuel pool. The Operator Aid Computer was out of       '
-
                service for replacement, and alignments for testing of containment
01.1 Loss of Spent Fuel Pool Coolina
                isolation valves in the component cooling water non-essential header
a. Insoection Scope (71707)
                were in progress. Inventory was inadvertently drained from the
On April 8. Unit 2 was in a refueling outage with all of the fuel off-
                component cooling water system over a seventy minute period. until the
loaded to the spent fuel pool.
                low-low level setpoint in the component cooling water surge tanks was
The Operator Aid Computer was out of
                reached. At this level, automatic isolation of the non-essential header
'
                occurred. the drain path was isolated, and cooling flow to the spent
service for replacement, and alignments for testing of containment
                fuel pool heat exchanger and pump motor cooler was isolated. 0]erators
isolation valves in the component cooling water non-essential header
                shutdown the pump to prevent overheating, initiated makeup to t1e
were in progress.
                component cooling water surge tanks. and closely monitored spent fuel
Inventory was inadvertently drained from the
                pool temperature. Spent fuel pool temperature increased to a maximum of
component cooling water system over a seventy minute period. until the
                108 F. within the TS limit. while operators determined the cause of the
low-low level setpoint in the component cooling water surge tanks was
                loss of component cooling water inventory and returned the non-essential
reached. At this level, automatic isolation of the non-essential header
occurred. the drain path was isolated, and cooling flow to the spent
fuel pool heat exchanger and pump motor cooler was isolated.
0]erators
shutdown the pump to prevent overheating, initiated makeup to t1e
component cooling water surge tanks. and closely monitored spent fuel
pool temperature. Spent fuel pool temperature increased to a maximum of
108 F. within the TS limit. while operators determined the cause of the
loss of component cooling water inventory and returned the non-essential
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                header to service.
header to service.
!
!
                As a result of the event, the licensee initiated Problem Investigation
As a result of the event, the licensee initiated Problem Investigation
                Process (PIP) report 2-C97-1090 and initiated a root cause evaluation
Process (PIP) report 2-C97-1090 and initiated a root cause evaluation
                that was performed by the Catawba Safety Review Group.
that was performed by the Catawba Safety Review Group.
                The inspector responded to the site upon notification of the loss of
The inspector responded to the site upon notification of the loss of
                spent fuel pool cooling: discussed the event with various personnel
spent fuel pool cooling: discussed the event with various personnel
                                                                      Enclosure 2
Enclosure 2
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    .   - -     .           - - .   _ -   . _   . . = - - . . - -.-. . . ~ . -                 .-
.
l                                                                                                    -
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      .
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- - .
_ -
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= - - . .
- -.-. . . ~ . -
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                  .
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                                                  2
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:                                                                                                     .
l
              involved; reviewed PT/2/A/4200/01T, Containment Penetration Valve
.
                Injection Water System Performance Test, approved 3/26/97: reviewed data
2
              on component cooling water surge tank level spent fuel pool cooling
:
              pump motor temperatures, and spent fuel pool temperature: and reviewed
.
              the root cause evaluation documented in the referenced PIP.
involved; reviewed PT/2/A/4200/01T, Containment Penetration Valve
            b. Observations and Findinas
Injection Water System Performance Test, approved 3/26/97: reviewed data
              At the time of the loss of spent fuel pool cooling, approximately 19                   -
on component cooling water surge tank level spent fuel pool cooling
              hours were available prior to boiling in the spent fuel pool. Operators                 I
pump motor temperatures, and spent fuel pool temperature: and reviewed
              methodically restored cooling within 1.5 hours, after identifying the
the root cause evaluation documented in the referenced PIP.
              cause, assessing equipment condition, and realigning the component                     .
b. Observations and Findinas
              cooling water system.                                                                   l
At the time of the loss of spent fuel pool cooling, approximately 19
              The licensee's root cause evaluation considered procedural adequacy.
-
              o]erator performance, ad supervisory oversight of the evolution. In
hours were available prior to boiling in the spent fuel pool. Operators
              taese areas, problems were identified and appropriate corrective actions
methodically restored cooling within 1.5 hours, after identifying the
              were delineated.
cause, assessing equipment condition, and realigning the component
              Procedure PT/2/A/4200/01T, Containment Penetration Valve Injection Water
.
              System Performance Test, included steps for the alignment of four
cooling water system.
              component cooling water containment penetrations that included valve
The licensee's root cause evaluation considered procedural adequacy.
  .
o]erator performance, ad supervisory oversight of the evolution.
              manipulation sequences that were incorrect. The incorrect sequences
In
              caused drain paths to be aligned through the inside containment
taese areas, problems were identified and appropriate corrective actions
              penetration vent on all four penetrations. The licensee's evaluation
were delineated.
              revealed that the Unit 1 procedure had similar errors. The errors
Procedure PT/2/A/4200/01T, Containment Penetration Valve Injection Water
              occurred during a process to convert engineering test procedures into
System Performance Test, included steps for the alignment of four
              the operations procedure format. Proposed corrective actions included a
component cooling water containment penetrations that included valve
              formal validation of the technical adequacy of other procedures that
manipulation sequences that were incorrect. The incorrect sequences
              have been or were to be converted. This procedure inadequacy, which
.
              caused the loss of spent fuel cooling constitutes a Violation (VIO) of
caused drain paths to be aligned through the inside containment
              TS 6.8.1. Procedures and Programs, and is identified as VIO 50-414/97-
penetration vent on all four penetrations. The licensee's evaluation
              07-01: Inadequate Procedure Resulting in Loss of Spent Fuel Pool
revealed that the Unit 1 procedure had similar errors. The errors
              Cooling with Core Off-loaded.
occurred during a process to convert engineering test procedures into
              The licensee's evaluation of operator performance concluded that the
the operations procedure format.
              equipment operator that performed the valve alignments appropriately
Proposed corrective actions included a
              questioned the high flow rate from the vent valves as they were opened,
formal validation of the technical adequacy of other procedures that
              but failed to stop and contact su3ervision when this unexpected response
have been or were to be converted. This procedure inadequacy, which
              was obtained. Also, the control aoard operators were not timely in
caused the loss of spent fuel cooling constitutes a Violation (VIO) of
              their assessment of an observed increased rate of input to the
TS 6.8.1. Procedures and Programs, and is identified as VIO 50-414/97-
              containment floor and equipment sump.
07-01:
              The inspector noted that the pre-job brief for performing the
Inadequate Procedure Resulting in Loss of Spent Fuel Pool
              containment Jenetration alignments was incomplete.             Personnel conducting
Cooling with Core Off-loaded.
              the pre-job arief did not emphasize that the component cooling water
The licensee's evaluation of operator performance concluded that the
equipment operator that performed the valve alignments appropriately
questioned the high flow rate from the vent valves as they were opened,
but failed to stop and contact su3ervision when this unexpected response
was obtained. Also, the control aoard operators were not timely in
their assessment of an observed increased rate of input to the
containment floor and equipment sump.
The inspector noted that the pre-job brief for performing the
containment Jenetration alignments was incomplete.
Personnel conducting
the pre-job arief did not emphasize that the component cooling water
i
i
              system was affected by the procedure and was being relied upon for
system was affected by the procedure and was being relied upon for
i
i
                                                                                  Enclosure 2
Enclosure 2


  .- --   .   -.         -       . .                 - - _ . .           . _ . -       ,     . - - - .
.- --
                                                                                                        i
.
            '
-.
        .
-
                            .
.
                                                                3
.
                        cooling the spent fuel pool with the core off-loaded. Also, the control
- - _ . .
                        room operators could have more diligently monitored this system, since
. _ .
                        it was performing an important function, and identified the decreasing
-
                        level in the component cooling water surge tanks before automatic
,
,                      actions occurred. Operations management had similar observations and
.
l                       took actions to imarove monitoring of systems performing important
- - -
                        functions during t1e remainder of the outage.
.
                    c. Conclusions
i
                                                                                                        ;
'
l                      The loss of spent fuel pool cooling was caused by an inadequate                 ;
.
.
3
cooling the spent fuel pool with the core off-loaded.
Also, the control
room operators could have more diligently monitored this system, since
it was performing an important function, and identified the decreasing
level in the component cooling water surge tanks before automatic
actions occurred. Operations management had similar observations and
,
l
took actions to imarove monitoring of systems performing important
functions during t1e remainder of the outage.
c. Conclusions
l
The loss of spent fuel pool cooling was caused by an inadequate
i
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                        containment penetration test procedure. Other barriers that could have
containment penetration test procedure.
                                                                                                        l
Other barriers that could have
!
prevented the event included increased emphasis on the importance of the
system function during the pre-job brief and more diligent control board
monitoring.
The operator's performance in response to the event was
appropriate. The Catawba Safety Review Group evaluation of the event
was detailed and identified substantive corrective actions.
01.2 Preoarations for Midlooo
!
!
                        prevented the event included increased emphasis on the importance of the
a. Insoection Scooe (71707)
                        system function during the pre-job brief and more diligent control board
l.
                        monitoring. The operator's performance in response to the event was
Near the conclusion of its refueling outage. Unit 2 entered midloo) on
                        appropriate. The Catawba Safety Review Group evaluation of the event
                        was detailed and identified substantive corrective actions.
                01.2 Preoarations for Midlooo
!
!
                    a. Insoection Scooe (71707)
April 23 for vacuum refill of the Reactor Coolant System (RCS). Tie
l.                      Near the conclusion of its refueling outage. Unit 2 entered midloo) on
i
!                      April 23 for vacuum refill of the Reactor Coolant System (RCS). Tie
inspector reviewed Generic Letter 88-17. Loss of Decay Heat Removal.
i                       inspector reviewed Generic Letter 88-17. Loss of Decay Heat Removal.
Catawba Nuclear Site Directive 3.1.30. Unit Shutdown Configuration
!
!
                        Catawba Nuclear Site Directive 3.1.30. Unit Shutdown Configuration
Control. Rev. 8. and the operating 3rocedures governing the RCS
                        Control. Rev. 8. and the operating 3rocedures governing the RCS
draindown to midloop, operation wit 1 reduced RCS inventory, and vacuum
,                      draindown to midloop, operation wit 1 reduced RCS inventory, and vacuum
,
                        refill. The inspector conducted control room observations during the             !
refill. The inspector conducted control room observations during the
                        draindown to midloop and portions of unit operation at midloop.
draindown to midloop and portions of unit operation at midloop.
                    b. Observations and Findinos
b. Observations and Findinos
                        The inspector verified that the requirements delineated in Catawba               l
The inspector verified that the requirements delineated in Catawba
                        Nuclear Site Directive 3.1.30 were satisfied. Specifically, multiple             :
Nuclear Site Directive 3.1.30 were satisfied.
                        thermocouples were available for temperature monitoring; ultrasonics and
Specifically, multiple
                        sightglass indications were available for level monitoring: vital power
thermocouples were available for temperature monitoring; ultrasonics and
                        was available from both offsite sources, as well as two emergency diesel
sightglass indications were available for level monitoring: vital power
                        generators; necessary emergency core cooling equipment was either
was available from both offsite sources, as well as two emergency diesel
                        operable or available: and the gravity flowpath criteria were satisfied
generators; necessary emergency core cooling equipment was either
                        for midloop operation with low decay heat.
operable or available: and the gravity flowpath criteria were satisfied
                        Just prior to reduced inventory operations, the inspector noticed that
for midloop operation with low decay heat.
                        valves 2ND-33. Residual Heat Removal (RHR) System Return to the
Just prior to reduced inventory operations, the inspector noticed that
                        Refueling Water Storage Tank (FWST). 2FW-27A and 2FW-55B. RHR Pumps 2A
valves 2ND-33. Residual Heat Removal (RHR) System Return to the
                        and 2B Suction from the FWST. were available as opposed to operable.
Refueling Water Storage Tank (FWST). 2FW-27A and 2FW-55B. RHR Pumps 2A
                        These valves are in the flowpaths of the three gravity feeds to the RCS.
and 2B Suction from the FWST. were available as opposed to operable.
                        The valves were tagged closed in support of RCS maintenance.       The
These valves are in the flowpaths of the three gravity feeds to the RCS.
The valves were tagged closed in support of RCS maintenance.
The
inspector questioned the a)proariateness of considering the associated
,
,
                        inspector questioned the a)proariateness of considering the associated
!
!                      flowpaths available with tie RiR and FWST valves closed under a tagout.
flowpaths available with tie RiR and FWST valves closed under a tagout.
;
;
Enclosure 2
!
!
                                                                                  Enclosure 2
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.
                .
.
l                                                 4
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                Normal makeup to the reactor coolant system via the chemical and volume
Normal makeup to the reactor coolant system via the chemical and volume
                control system was available.
control system was available.
l               The inspector inquired about the status of the RHR and FWST valves
l
                during reduced inventory and midloo) operations and determined that.
The inspector inquired about the status of the RHR and FWST valves
,              although they were tagged closed, t1e Work Control Center filed the tags
during reduced inventory and midloo) operations and determined that.
l               in a prominent location to facilitate equipment restoration in the event
although they were tagged closed, t1e Work Control Center filed the tags
l             that these valves were needed to mitigate a loss of RHR.
,
l
in a prominent location to facilitate equipment restoration in the event
l
that these valves were needed to mitigate a loss of RHR.
:
:
              The inspector reviewed Catawba Nuclear Site Directive 3.1.30 to
The inspector reviewed Catawba Nuclear Site Directive 3.1.30 to
              determine if administrative requirements were being met. The directive
determine if administrative requirements were being met. The directive
                stated that, for midloop operations with low decay heat load, two       ;
stated that, for midloop operations with low decay heat load, two
;
available gravity flowpaths were required. The directive defines
l
"available" as "the status of a system, structure or component that is
'
in service or can be placed in service in a functional or operable state
by immediate manual or automatic actuation." The directive considers
actions taken by operators to clear tags acceptable for restoring
,
equipment to functional or operable status within a reasonable period of
time.
l
l
                available gravity flowpaths were required. The directive defines        i
The inspector raised a concern to the licensee that, while valves 2FW-
                "available" as "the status of a system, structure or component that is  '
27A. 2FW-55B. and 2ND-33 could possibly be restored to service in a
                in service or can be placed in service in a functional or operable state i
reasonable period of time, other components that might be impacted by
              by immediate manual or automatic actuation." The directive considers      !
.
                actions taken by operators to clear tags acceptable for restoring        ,
the maintenance activity in progress might not be accounted for before
              equipment to functional or operable status within a reasonable period of  l
the gravity flowpath would be utilized.
              time.
Hence, points of compromised
                                                                                        l
'
              The inspector raised a concern to the licensee that, while valves 2FW-
system integrity, which could allow flow to be diverted from the RCS.
              27A. 2FW-55B. and 2ND-33 could possibly be restored to service in a
might be overlooked and either reduce the assumed flow to the RCS or
  .
!
              reasonable period of time, other components that might be impacted by
extend the amount of time needed to place the gravity flowpath in
              the maintenance activity in progress might not be accounted for before   ;
service.
              the gravity flowpath would be utilized. Hence, points of compromised     '
Although no such conditions were identified during the midloop
              system integrity, which could allow flow to be diverted from the RCS.
and vacuum refill evolutions, the licensee plans to evaluate Nuclear
              might be overlooked and either reduce the assumed flow to the RCS or     !
Site Directive 3.1.30 to determine if changes are warranted prior to the
              extend the amount of time needed to place the gravity flowpath in
next refueling outage.
              service. Although no such conditions were identified during the midloop
c. Conclusions
              and vacuum refill evolutions, the licensee plans to evaluate Nuclear
The inspector concluded that the draindown to midloop, midloop
              Site Directive 3.1.30 to determine if changes are warranted prior to the
operation, and vacuum refill were conducted without incident.
              next refueling outage.
In
          c. Conclusions
general, the licensee implements effective controls for these
              The inspector concluded that the draindown to midloop, midloop
.
              operation, and vacuum refill were conducted without incident. In
evolutions.
              general, the licensee implements effective controls for these
However, the inspector questioned the availability of
                                                                                        .
1
                                                                                        ;
equipment required for gravity flow to the core and expressed concern
              evolutions. However, the inspector questioned the availability of         1
that the process for restoring needed equipment may not be sufficiently
              equipment required for gravity flow to the core and expressed concern
controlled.
              that the process for restoring needed equipment may not be sufficiently
01.3 Doerator Aid Comouter Installation and Comoensatory Action
              controlled.
a. Insoection Scooe (71707)
        01.3 Doerator Aid Comouter Installation and Comoensatory Action
l
          a. Insoection Scooe (71707)
During the Operator Aid Computer (OAC) installation, the inspector
l             During the Operator Aid Computer (OAC) installation, the inspector
;
;             periodically verified that the Loss of DAC procedure was implemented
periodically verified that the Loss of DAC procedure was implemented
l             while the OAC was unavailable.     The inspector observed an open main
l
                                                                        Enclosure 2
while the OAC was unavailable.
The inspector observed an open main
(
(
Enclosure 2


                  .           .   .-       _-       .             ._     _ -   - - . -
.
      '
.
.-
_-
.
._
_ -
- - .
-
1
1
    .
'
              .
.
                                                5                                 ,
.
            control room door and reviewed the associated compensatory action.
5
            " Control Room Pressure Boundary." dated March 20. 1997, to verify that
,
            the licensee had satisfied selected initial conditions that allowed the
control room door and reviewed the associated compensatory action.
            door to remain open. The inspector also evaluated the licensee's
" Control Room Pressure Boundary." dated March 20. 1997, to verify that
            im)lementation of the compensatory action guidance following receipt of
the licensee had satisfied selected initial conditions that allowed the
            a Jnit 2 fuel handling building high radiation alarm that occurred on
door to remain open.
            March 24.
The inspector also evaluated the licensee's
        b. Observations and Findinas
im)lementation of the compensatory action guidance following receipt of
            During the Unit 2 OAC installation. the OAC was not available for               <
a Jnit 2 fuel handling building high radiation alarm that occurred on
l           automatic surveillance of numerous plant parameters. As a result, the           I
March 24.
            control room operators were required to implement PT/1/A/4600/09. Loss
b. Observations and Findinas
            of Operator Aid Computer, and perform those surveillances manually'on
During the Unit 2 OAC installation. the OAC was not available for
            specified time intervals. The inspector periodically verified that the         l
<
            procedure was in use while OAC monitoring was unavailable. Often a             l
l
            dedicated reactor operator was available to perform this function.
automatic surveillance of numerous plant parameters. As a result, the
control room operators were required to implement PT/1/A/4600/09. Loss
of Operator Aid Computer, and perform those surveillances manually'on
specified time intervals. The inspector periodically verified that the
procedure was in use while OAC monitoring was unavailable. Often a
dedicated reactor operator was available to perform this function.
;
;
although that could not always be accommodated.
The inspector
determined that the procedure was in place and being implemented when
'
'
            although that could not always be accommodated. The inspector
required.
            determined that the procedure was in place and being implemented when
l
            required.
The inspector observed that the Unit 2 control room vital access door
l           The inspector observed that the Unit 2 control room vital access door
was opened on March 22 and was left open continuously to allow passage
            was opened on March 22 and was left open continuously to allow passage
'
'
  .
            of a flexible ventilation duct (approx. 12 inch diameter). The duct was
.
.
of a flexible ventilation duct (approx. 12 inch diameter). The duct was
.
used to exhaust fumes generated from welding performed to install the
I
I
            used to exhaust fumes generated from welding performed to install the
replacement operator aid computer in the Unit 2 main control board
            replacement operator aid computer in the Unit 2 main control board
panel. The inspector discussed the compensatory actions with
            panel. The inspector discussed the compensatory actions with
engineering and operations 3ersonnel to determine if the compensatory
            engineering and operations 3ersonnel to determine if the compensatory
actions would ensure that tie control room would pressurize sufficiently
            actions would ensure that tie control room would pressurize sufficiently
to meet control room habitability requirements during design basis
'
'
            to meet control room habitability requirements during design basis
events.
            events. Both operations and engineering personnel stated the design
Both operations and engineering personnel stated the design
            basis for contrM room pressurization and habitability would be met
basis for contrM room pressurization and habitability would be met
            provided that initic1 conditions of the compensatory action were
provided that initic1 conditions of the compensatory action were
            satisfied and that the control room door would be manually closed, after
satisfied and that the control room door would be manually closed, after
            separating a connection in the duct. if certain plant events (e.g..
separating a connection in the duct. if certain plant events (e.g..
            safety injection signal) were to occur.
safety injection signal) were to occur.
            The inspector verified that selected initial conditions were satisfied
The inspector verified that selected initial conditions were satisfied
            and found no discrepancies with the plant conditions that existed at the
and found no discrepancies with the plant conditions that existed at the
            time of the inspection. The inspector observed, however, that the
time of the inspection.
            initial conditions of the compensatory action were not being
The inspector observed, however, that the
            periodically verified to ensure that plant changes since the initial
initial conditions of the compensatory action were not being
            condition verification on March 22 had not invalidated the assumptions
periodically verified to ensure that plant changes since the initial
            supporting the compensatory action. Operations personnel informed the
condition verification on March 22 had not invalidated the assumptions
            inspector that periodic verification of initial conditions for the
supporting the compensatory action. Operations personnel informed the
            compensatory actions was not required.
inspector that periodic verification of initial conditions for the
l          The inspector expressed a concern to the licensee that, because there
compensatory actions was not required.
l
l
            was a high number of initial conditions required for this particular
The inspector expressed a concern to the licensee that, because there
            compensatory action and because of the relatively long duration of the
l
was a high number of initial conditions required for this particular
compensatory action and because of the relatively long duration of the
:
:
                                                                    Enclosure 2
Enclosure 2
1
1


    ..   -         .                     .       . ..     . - -   --         . - - - -
..
          '
-
      .
.
                      .
.
!                                                         6
.
..
. - -
--
. - - - -
'
.
.
!
6
replacement operator aid com) uter installation, periodic verification of
l
l
                      replacement operator aid com) uter installation, periodic verification of
initial conditions may have 3een warranted to ensure that necessary
                      initial conditions may have 3een warranted to ensure that necessary
conditions continued to be met.
                      conditions continued to be met. Additionally, the licensee recognized
Additionally, the licensee recognized
                      that changes in plant ventilation equipment status created by refueling
that changes in plant ventilation equipment status created by refueling
                    outage activities could invalidate the assumptions of the analysis
outage activities could invalidate the assumptions of the analysis
                    supporting the compensatory action.
supporting the compensatory action.
                                                                                                l
The licensee initiated timely corrective actions to periodically
                    The licensee initiated timely corrective actions to periodically           l
reverify the initial conditions of the compensatory action.
                      reverify the initial conditions of the compensatory action. The           i
The
i
,
,
                    periodicity of the reverification varied based on the potential for the     !
periodicity of the reverification varied based on the potential for the
l
l
                    condition to change. The inspector observed the reverification of the     -
condition to change.
                      initial conditions following implementation of the licensee's corrective
The inspector observed the reverification of the
                    actions.
-
initial conditions following implementation of the licensee's corrective
actions.
l
l
The inspector observed two other minor discreaancies during the review
,
,
                    The inspector observed two other minor discreaancies during the review
of the compensatory action im)lementation.
                    of the compensatory action im)lementation. T1e control room door was
T1e control room door was
i                   not closed on March 24 when tie Unit 2 spent fuel pool bridge radiation     i
i
                    monitor (2 EMF 4) alarmed although this appeared to be a condition for       l
not closed on March 24 when tie Unit 2 spent fuel pool bridge radiation
;                   closing the door. The inspector determined that the radiological
i
;                   conditions that caused the alarm were inconsequential and not related to   ;
monitor (2 EMF 4) alarmed although this appeared to be a condition for
;
closing the door.
The inspector determined that the radiological
;
conditions that caused the alarm were inconsequential and not related to
l
l
                    a release (refer to Section 01.5). The inspector also found that the
a release (refer to Section 01.5).
                    accountability log sheet that specified individuals responsible for
The inspector also found that the
  .
accountability log sheet that specified individuals responsible for
                    manually closing the control room door had not been signed for one day.
manually closing the control room door had not been signed for one day.
                    The inspector determined that the individuals involved were aware of
.
l                  their responsibilities, but had committed an administrative error.          <
The inspector determined that the individuals involved were aware of
                    The licensee documented the inspector's concerns in Problem
                      Investigation Process (PIP) Report 0-C97-0988 and initiated actions to
l
l
                    determine: (1) if the response to the alarm was appropriate: (2) the
their responsibilities, but had committed an administrative error.
<
The licensee documented the inspector's concerns in Problem
Investigation Process (PIP) Report 0-C97-0988 and initiated actions to
l
determine:
(1) if the response to the alarm was appropriate: (2) the
cause of the administrative error: and (3) if a reverification process
'
'
                    cause of the administrative error: and (3) if a reverification process
;
;                    for compensatory actions is needed.
for compensatory actions is needed.
I               c. Conclusions
I
                  The inspector concluded that control room operators were appropriately
c. Conclusions
l                  implementing their procedure for Loss of OAC when the OAC was
The inspector concluded that control room operators were appropriately
                    unavailable during the installation process. Additionally, operator
implementing their procedure for Loss of OAC when the OAC was
                    effectiveness in implementing a complex compensatory action was
l
                  challenged by numerous initial conditions and the lack of periodic
unavailable during the installation process. Additionally, operator
                    reverification to ensure that they were being continuously met.
effectiveness in implementing a complex compensatory action was
            01.4 Boron Dilution Mitiaation System Reliability
challenged by numerous initial conditions and the lack of periodic
                a. Insoection Scope (71707)
reverification to ensure that they were being continuously met.
                  Du' ring the Unit 2 shutdown for refueling outage 2E0C8. multiple problems
01.4 Boron Dilution Mitiaation System Reliability
,                  associated with the Boron Dilution Mitigation System (BDMS) were
a. Insoection Scope (71707)
                  encountered. The inspector investigated the nature of each problem and
Du' ring the Unit 2 shutdown for refueling outage 2E0C8. multiple problems
                    reviewed the work history of the BDMS for both units. The inspector
associated with the Boron Dilution Mitigation System (BDMS) were
,
encountered.
The inspector investigated the nature of each problem and
reviewed the work history of the BDMS for both units. The inspector
i
i
                                                                            Enclosure 2
Enclosure 2
l
l
l
l
Line 612: Line 820:
!
!


  -             .       .     . - _     - . - .   - -     . ..           . - - .. ..
-
                                                                                          !
.
      .                                                                                   !
.
    ,
.
                                                  7                                     l
- _
            reviewed the FSAR and Technical Specifications (TS) and discussed system
- . - .
          performance and vulnerabilities with engineering personnel.
-
-
.
..
. - -
..
..
!
.
!
,
7
l
reviewed the FSAR and Technical Specifications (TS) and discussed system
performance and vulnerabilities with engineering personnel.
b. Observations and Findinas
,
,
        b. Observations and Findinas
The BDMS consists of two trains and is designed to protect the reactor
          The BDMS consists of two trains and is designed to protect the reactor         .
.
            from an inadvertent criticality by automatically stopping the flow of         i
from an inadvertent criticality by automatically stopping the flow of
          unborated water to the core during shutdown conditions. Required by TS
i
            in Modes 3, 4. 5. and 6. the BDMS uses two source range detectors to         '
unborated water to the core during shutdown conditions.
          monitor the subcritical multiplication of the reactor core. An alarm           ,
Required by TS
          set)oint is continually calculated, and if the setpoint is exceeded,
in Modes 3, 4. 5. and 6. the BDMS uses two source range detectors to
          eitler train of BDMS will automatically shut off both reactor makeup
'
          water pumps, align the suction of the charging pumps to the Refueling
monitor the subcritical multiplication of the reactor core.
          Water Storage Tank (FWST), and isolate flow to the charging pumps from         .
An alarm
          the Volume Control Tank.     Because these functions are automated, no
,
          operator action is required.
set)oint is continually calculated, and if the setpoint is exceeded,
          Technical Specification 3.9.2 requires both trains of the BDMS to be
eitler train of BDMS will automatically shut off both reactor makeup
          operable during Mode 6.     If one or bcth trains are inoperable, the
water pumps, align the suction of the charging pumps to the Refueling
          licensee must either suspend core alterations or verify' that source           +
Water Storage Tank (FWST), and isolate flow to the charging pumps from
          range neutron flux monitors are operable with alarm setpoints
.
          a)propriately calculated for the current (and, during core reload,
the Volume Control Tank.
          clanging) steady-state count rate. The licensee also must take
Because these functions are automated, no
          additional actions to verify that audible alarms are available in the
operator action is required.
          control room and containment, and that reactor makeup water pump flow
Technical Specification 3.9.2 requires both trains of the BDMS to be
          rates are within limits. In addition the BDMS is required operable
operable during Mode 6.
          during Modes 3, 4 and 5 by TF 3.3.3.11.
If one or bcth trains are inoperable, the
          kDuringtheUnit2refuelingoutage,multipleproblemswiththeBDMSwere
licensee must either suspend core alterations or verify' that source
          encountered. On March 25. Unit 2 BDMS interlock testing revealed a
+
          failure to secure the reactor makeup water pumps. The failure was
range neutron flux monitors are operable with alarm setpoints
          attributed to a failed optical isolator. On March 28 during core
a)propriately calculated for the current (and, during core reload,
          offload to the Spent Fuel Pool, a spike on the B train source range
clanging) steady-state count rate.
          instrument caused the charging pump suction to swap from the Volume
The licensee also must take
          Control Tank to the FWST.' This spike was attributed to noise generated
additional actions to verify that audible alarms are available in the
          by welding activities during the Operator Aid Computer replacement and
control room and containment, and that reactor makeup water pump flow
          exacerbated by a loose plug at the data processing cabinet. A third
rates are within limits.
          problem, which also occurred during the core offload, was associated
In addition the BDMS is required operable
          with a shutdown monitor that failed to a zero signal reading. Because
during Modes 3, 4 and 5 by TF 3.3.3.11.
          of the latter two problems the BDMS was declared inoperable, and the
kDuringtheUnit2refuelingoutage,multipleproblemswiththeBDMSwere
          required TS actions were performed.
encountered. On March 25. Unit 2 BDMS interlock testing revealed a
          Problems with the BDMS had been encountered periodically in the past.
failure to secure the reactor makeup water pumps.
          According to the licensee's Work Management System (WMS), numerous work
The failure was
          requests have been written since 1987 for the BDMS. Since 1986. 134
attributed to a failed optical isolator.
          work requests have been closed for the Unit 1 BDMS: since 1987. 83 work
On March 28 during core
          requests have been closed for the Unit 2 BDMS. The inspector could not
offload to the Spent Fuel Pool, a spike on the B train source range
          consistently determine if specific work requesis were generated to
instrument caused the charging pump suction to swap from the Volume
          resolve system problems or if they were "onerated for other reasons
Control Tank to the FWST.' This spike was attributed to noise generated
          (e.g. nameplate installation). Nonetheles:.. the volume of work requests
by welding activities during the Operator Aid Computer replacement and
                                                                    Enclosure 2
exacerbated by a loose plug at the data processing cabinet. A third
                                                                                          ,
problem, which also occurred during the core offload, was associated
                                                                                          k
with a shutdown monitor that failed to a zero signal reading.
                                                                                          b
Because
of the latter two problems the BDMS was declared inoperable, and the
required TS actions were performed.
Problems with the BDMS had been encountered periodically in the past.
According to the licensee's Work Management System (WMS), numerous work
requests have been written since 1987 for the BDMS.
Since 1986. 134
work requests have been closed for the Unit 1 BDMS: since 1987. 83 work
requests have been closed for the Unit 2 BDMS. The inspector could not
consistently determine if specific work requesis were generated to
resolve system problems or if they were "onerated for other reasons
(e.g. nameplate installation).
Nonetheles:.. the volume of work requests
Enclosure 2
,
k
b


                                      '
                                                                                              t
l
l
      .-                                                                                    ;
'
  '
L                                                                                            !
l                  -
                                                                                              ,
                                                    8                                        !
                                                                                            i
                  related to this system seemed high.    The inspector expressed to the      t
l                licensee a concern with BDMS reliability and availability, as well as
                  the resulting impact (i.e., additional calibrations and monitoring) to
l                control room operators. The licensee had come to the same conclusion        *
                through a system review independent of the NRC's inspection. Based on        !
                  their findings, the licensee had recently decided to incorporate the        !
                  BDMS into the site's Top Equipment Problem Resolution (TEPR) program.      l
            c. Conclusions
t
t
.-
;
'
'
                  Problems encountered with the BDMS during the' Unit 2 refueling outage
L
                . were indicative of historical system performance problems, which affect     ;
!
                plant operation during modes 3. 4. 5 and 6. The inspector concluded           I
l
                that, since additional monitoring and calibration activities are
-
    ~            required when the BDMS is inoperable the BDMS has caused additional
,
                  control room operator workload to compensate for its unreliability. The
8
i-                licensee has indicated that efforts are being initiated to improve
!
                  system reliability and, thereby. reduce operator burden through the TEPR
i
                process. So that the licensee's efforts to correct this adverse system
related to this system seemed high.
The inspector expressed to the
t
l
licensee a concern with BDMS reliability and availability, as well as
the resulting impact (i.e., additional calibrations and monitoring) to
l
control room operators. The licensee had come to the same conclusion
*
through a system review independent of the NRC's inspection.
Based on
!
their findings, the licensee had recently decided to incorporate the
!
BDMS into the site's Top Equipment Problem Resolution (TEPR) program.
l
c. Conclusions
t
Problems encountered with the BDMS during the' Unit 2 refueling outage
'
. were indicative of historical system performance problems, which affect
;
plant operation during modes 3. 4. 5 and 6.
The inspector concluded
that, since additional monitoring and calibration activities are
required when the BDMS is inoperable the BDMS has caused additional
~
control room operator workload to compensate for its unreliability. The
licensee has indicated that efforts are being initiated to improve
i-
system reliability and, thereby. reduce operator burden through the TEPR
process.
So that the licensee's efforts to correct this adverse system
.
.
performance trend can be monitored to resolution, this issue is
'
'
                performance trend can be monitored to resolution, this issue is
identified as Inspector Followup Item 50-413.414/97-07-02: Boron
                  identified as Inspector Followup Item 50-413.414/97-07-02: Boron
Dilution Mitigation System Reliability Resolution.
                Dilution Mitigation System Reliability Resolution.
:.
:.
          01.5 Fuel Handlino Buildina Evacuation
01.5 Fuel Handlino Buildina Evacuation
            a. Insoection Scooe (71707)
a. Insoection Scooe (71707)
                'The inspector evaluated the licensee's response to a radiation alarm
'The inspector evaluated the licensee's response to a radiation alarm
                  resulting in an evacuation of the fuel handling building that occurred
resulting in an evacuation of the fuel handling building that occurred
                on March 24. The inspector reviewed licensee's procedures, conducted
on March 24. The inspector reviewed licensee's procedures, conducted
                interviews with involved personnel, and walked down the fuel handling
interviews with involved personnel, and walked down the fuel handling
                building.
building.
            b. Observations and Findinas
b. Observations and Findinas
                On March-24. the inspector responded to the control room when the               ,
On March-24. the inspector responded to the control room when the
                control room operators announced over the public address system the           i
control room operators announced over the public address system the
                evacuation of the fuel handling building. During this time, the water
i
                                                                                                '
,
                level in the fuel transfer canal had been lowered to facilitate
evacuation of the fuel handling building.
                maintenance on valve 2KF-122. Fuel Transfer Canal Isolation Valve. The
During this time, the water
                ins)ector found that the spent' fuel pool bridge radiation detector
                  (2EiF-4) had alarmed, and annunciator response procedure for alarm 2-
                RAD-3 had been implemented. The control room o)erators conservatively
                elected.to evacuate the fuel handling building )ecause the ah:r.m was not    ;
                expected.- The inspector verified that the control room operators            i
;                properly followed their procedures and that the appropriate level of          I
                supervisory oversight was maintained during the event.                      j
'
'
                The inspector also discussed the event with Radiation Protection               '
level in the fuel transfer canal had been lowered to facilitate
                personnel and found that proper actions were completed. Radiation
maintenance on valve 2KF-122. Fuel Transfer Canal Isolation Valve. The
                                                                          Enclosure 2
ins)ector found that the spent' fuel pool bridge radiation detector
                                                                                                !
(2EiF-4) had alarmed, and annunciator response procedure for alarm 2-
                                                                                                I
RAD-3 had been implemented. The control room o)erators conservatively
                                .   -                     -
elected.to evacuate the fuel handling building )ecause the ah:r.m was not
                                                                    -       _       -   .
expected.- The inspector verified that the control room operators
i
;
properly followed their procedures and that the appropriate level of
supervisory oversight was maintained during the event.
j
'
The inspector also discussed the event with Radiation Protection
'
personnel and found that proper actions were completed.
Radiation
Enclosure 2
!
I
.
-
-
-
_
-
.


    ._   . _ _ _ _ _ _ _ . -                   _.._ _._.     -e.__________...-                               _._ _
._
                                                                                                                    t
. _ _ _ _ _ _ _ . -
                                                                                                                    ;
_.._ _._.
                *
-e.__________...-
i'     .                                                                                                           i
_._
                                  .                                                                                 i
_
!                                                                       9                                           {
t
;
*
i'
i
.
.
i
!
9
{
!
!
Protection technicians surveyed the area and reported back to the
;
control room.
Subsequently, the 2FME-4 alarm setpoint was raised to
2
three times the background radiation level in'accordance with approved
!
procedures.
Additionally, the inspector verified that the area survey
:
map for the fuel handling building was updated, and the associated
i
instrument log for 2 EMF-4 was changed to reflect-the new setpoint.
!
l
Because the alarm was not anticipated, the licensee initiated actions to
i
evaluate the root cause of the event and determine appropriate
l
corrective action.
Discussions with various plant )ersonnel revealed
'
that better coordination between affected plant wort groups and a
!
possible procedure enhancement were needed during fuel transfer canal
i
draining. This would provide for an increase in the alarm setpoint to
i
accommodate the expected increase in background radiation levels in the
i
!
!
                                                                                                                    !
area with the canal drained.
                                  Protection technicians surveyed the area and reported back to the                ;
                                control room. Subsequently, the 2FME-4 alarm setpoint was raised to                2
                                three times the background radiation level in'accordance with approved            !
                                procedures.        Additionally, the inspector verified that the area survey      :
                                map for the fuel handling building was updated, and the associated                i
                                instrument log for 2 EMF-4 was changed to reflect-the new setpoint.                !
                                                                                                                    l
                                Because the alarm was not anticipated, the licensee initiated actions to          i
                                evaluate the root cause of the event and determine appropriate                    l'
                                corrective action. Discussions with various plant )ersonnel revealed
                                that better coordination between affected plant wort groups and a                  !
                                possible procedure enhancement were needed during fuel transfer canal               i
                                draining. This would provide for an increase in the alarm setpoint to              i
!
!
                                accommodate the expected increase in background radiation levels in the            i
On March 25. the inspector performed a walkdown of the fuel handling
                                area with the canal drained.
building for area familiarization.
!                                On March 25. the inspector performed a walkdown of the fuel handling               !
During the walkdown the inspector
                                building for area familiarization. During the walkdown the inspector               '
performed a housekeeping assessment with emphasis on the licensee's
                                performed a housekeeping assessment with emphasis on the licensee's
'
adherence to foreign material exclusion (FME) requirements. ' The
>
>
                                adherence to foreign material exclusion (FME) requirements. ' The                  :
:
l                               inspector found that miscellaneous items (e.g. safety belt, tool bag,             2
l
                                face shield. grease gun, and paper) i.ere on the transfer canal catwalk             :
inspector found that miscellaneous items (e.g. safety belt, tool bag,
  .
2
                                area and had not been logged into the cleanliness logbook. The licensee             i
face shield. grease gun, and paper) i.ere on the transfer canal catwalk
                                subsequently issued PIP 2-C97-08/1 to document this NRC observation and
:
                                                                                                                    i
area and had not been logged into the cleanliness logbook. The licensee
                                address corrective actions.                                                         '
i
                                                                                                                    i
.
                            c. Conclusions
subsequently issued PIP 2-C97-08/1 to document this NRC observation and
                                                          .
i
                                                                                                                    L
address corrective actions.
                                The inspector concluded that actions by operations and RP personnel .in             '
'
l                               response to the radiation alarm in the fuel handling building were good.             "
i
!                               However, administrative controls over FME were not pro)erly im)1emented
c. Conclusions
t                                by personnel working near the fel transfer canal in t1e fuel landling
.
                                building.
L
                      01.6 Unit 1 Pressurizer Block Valve Control Circuit Failure
The inspector concluded that actions by operations and RP personnel .in
                            a. Insaection Scone (71707. 61726. 62707)
'
                                                                                                                    '
l
                                On March 20, Unit 1 pressurizer Power 0)erated Relief Valve (PORV) block
response to the radiation alarm in the fuel handling building were good.
                                valve INC-33A failed.to. stroke closed w1en the valve control switch was
"
                                placed in the closed position during surveillance testing. A similar
!
                                failure of this valve had occurred on August 10, 1995. The inspector
However, administrative controls over FME were not pro)erly im)1emented
                                reviewed the licensee's immediate actions to comply with TS action
by personnel working near the fel transfer canal in t1e fuel landling
                                requirements and an associated operability evaluation. The inspector
t
                                also reviewed PIP documentation (1-C97-0781 and 1-C95-1204) and the
building.
                                licensee's evaluation of the potential repeat failure.
01.6 Unit 1 Pressurizer Block Valve Control Circuit Failure
a. Insaection Scone (71707. 61726. 62707)
'
On March 20, Unit 1 pressurizer Power 0)erated Relief Valve (PORV) block
valve INC-33A failed.to. stroke closed w1en the valve control switch was
placed in the closed position during surveillance testing. A similar
failure of this valve had occurred on August 10, 1995. The inspector
reviewed the licensee's immediate actions to comply with TS action
requirements and an associated operability evaluation. The inspector
also reviewed PIP documentation (1-C97-0781 and 1-C95-1204) and the
licensee's evaluation of the potential repeat failure.
'
'
.
.
:
:
!
!
:-                                                                                             Enclosure 2
:-
                      . - .                 ,                       -.   .                 .
Enclosure 2
. - .
,
-.
.
.
-


                                          - _         _ _   ._           __
- _
      *
_
    ,
_
                                                                                          I
._
                                                                                          i
__
                                                  10
*
          b. Observations and Findinos
,
              The block valve is controlled with a three position control switch
i
                (open/close/ override). During the surveillance test the valve failed to
10
              close when the "close" Josition was selected. The licensee declared the   -
b. Observations and Findinos
              valve inoperable and suasequently succeeded in closing the valve using
The block valve is controlled with a three position control switch
                                                                                          '
(open/close/ override).
              the " override" position. The inspector verified that the licensee met     .
During the surveillance test the valve failed to
              TS requirements after the valve was declared inoperable (TS 3.4.4.
close when the "close" Josition was selected.
              Relief Valves).
The licensee declared the
              Maintenance troubleshooting determined that the failure occurred in an
-
              interlock portion of the block valve's control circuit. The interlock     ;
valve inoperable and suasequently succeeded in closing the valve using
              uses position signals generated from stem mounted limit switches located   ,
'
              on the two other Unit 1 pressurizer PORV block valves. An operability     l
the " override" position.
              evaluation performed after troubleshooting efforts concluded that the       ;
The inspector verified that the licensee met
              block valve was operable since it would remain capable of closing as
TS requirements after the valve was declared inoperable (TS 3.4.4.
              required using the " override" position. The licensee's investigation of   l
.
                                                                                          .
Relief Valves).
              the previous failure in 1995 found that a limit switch lever shaft had
Maintenance troubleshooting determined that the failure occurred in an
              broken. The licensee has scheduled work orders to inspect the limit
interlock portion of the block valve's control circuit. The interlock
              switches and block valves during the next refueling outage and will
uses position signals generated from stem mounted limit switches located
              initiate further investigation if the same type of failure has occurred.   J
,
  .        c. Conclusions                                                               '
on the two other Unit 1 pressurizer PORV block valves. An operability
              A Unit 1 pressurizer PORV block valve control circuit failure occurred
evaluation performed after troubleshooting efforts concluded that the
              which is a potential repeat of a previous 1995 failure. The licensee
block valve was operable since it would remain capable of closing as
                                                                                          .
required using the " override" position.
                                                                                        I
The licensee's investigation of
              has planned appropriate actions to determine the cause of the control       '
.
              circuit component failure when the components are accessible at the next
the previous failure in 1995 found that a limit switch lever shaft had
              refueling outage.
broken.
        08   Miscellaneous Operations Issues (92901. 92902)
The licensee has scheduled work orders to inspect the limit
        08.1   (Closed) VIO 50-413.414/94-13-01: Failure To Follow Procedure NSD 703     4
switches and block valves during the next refueling outage and will
              And Station Directive 34.0.5 Requirements.
initiate further investigation if the same type of failure has occurred.
              The inspectors reviewed the corrective actions identified by the
J
              licensee for this violation in letters dated August 15. 1994, and August
c. Conclusions
              8.1995, and verified that these actions were reasonable and complete.
'
              The licensee's evaluation substantiated the violation and identified       '
.
              approximately 600 comaonents which were provided with an identification     '
A Unit 1 pressurizer PORV block valve control circuit failure occurred
              tag that identified t1e component number, but the tag did not include
.
              the component's noun name as required by the site's procedures. The
which is a potential repeat of a previous 1995 failure. The licensee
              inspectors performed a sample inspection of these components and           !
has planned appropriate actions to determine the cause of the control
              verified that the identification tag included both the component number
'
              and noun name.                                                             4
circuit component failure when the components are accessible at the next
                                                                                          l
refueling outage.
08
Miscellaneous Operations Issues (92901. 92902)
08.1
(Closed) VIO 50-413.414/94-13-01: Failure To Follow Procedure NSD 703
4
And Station Directive 34.0.5 Requirements.
The inspectors reviewed the corrective actions identified by the
licensee for this violation in letters dated August 15. 1994, and August
8.1995, and verified that these actions were reasonable and complete.
The licensee's evaluation substantiated the violation and identified
'
approximately 600 comaonents which were provided with an identification
'
tag that identified t1e component number, but the tag did not include
the component's noun name as required by the site's procedures. The
inspectors performed a sample inspection of these components and
verified that the identification tag included both the component number
and noun name.
4
l
l
!
!
                                                                      Enclosure 2
Enclosure 2
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l
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l
Line 854: Line 1,189:
l
l


      -     __         _ _ _     _         ._     __ _         _ _ _ _ _ _   _ _ _ _     __
-
                                                                                                ,
__
        *
_ _ _
    .
_
                      .
._
                                                          11
__ _
          08.2 (Closed) VIO 50-413/95-07-01: Inadequate Modification Procedure
_ _ _ _ _ _
                    Resulting in Loss of RHR.
_ _ _ _
                    TN/1/A/1331/00/01A. Procedure for the Implementation of NSM CN-11331.
__
                    Work Unit 01. did not receive adequate cross disciplinary review to
,
                    determine operational impact and scheduling to determine a safe plant
*
                    condition for implementation. The licensee's response dated April 28,
.
                    1995. stated that immediate actions were taken to revise the procedure
.
                    and stop work on modification implementation until all modification
11
                    packages were reviewed for similar errors. Additionally, the licensee
08.2 (Closed) VIO 50-413/95-07-01: Inadequate Modification Procedure
                    formed two self-assessment teams to determine root cause of the event.
Resulting in Loss of RHR.
                    The modification process was also revised to add new screening criteria     I
TN/1/A/1331/00/01A. Procedure for the Implementation of NSM CN-11331.
                    for critical modifications that require an independent Senior Reactor       1
Work Unit 01. did not receive adequate cross disciplinary review to
                    0)erator review to determine safe plant conditions for implementation of     i
determine operational impact and scheduling to determine a safe plant
                    t1ese modifications. The inspector reviewed corrective action               j
condition for implementation. The licensee's response dated April 28,
                    documentation (PIP 1-C95-0203) and verified that the licensee completed
1995. stated that immediate actions were taken to revise the procedure
                    these actions.
and stop work on modification implementation until all modification
          08.3 (Closed) VIO 50-413.414/95-07-02: Inadequate Valve Verification
packages were reviewed for similar errors. Additionally, the licensee
                    Activities - Two Examples.
formed two self-assessment teams to determine root cause of the event.
The modification process was also revised to add new screening criteria
for critical modifications that require an independent Senior Reactor
1
0)erator review to determine safe plant conditions for implementation of
t1ese modifications.
The inspector reviewed corrective action
j
documentation (PIP 1-C95-0203) and verified that the licensee completed
these actions.
08.3 (Closed) VIO 50-413.414/95-07-02: Inadequate Valve Verification
Activities - Two Examples.
l
l
Both examples of the violation involved personnel that failed to use
proper verification methods or independent verification of determining
.
l
valve position or valve location.
The licensee's response dated April
l
l
l                    Both examples of the violation involved personnel that failed to use
!
  .
28, 1995, stated that procedure revisions and additional training was
                    proper verification methods or independent verification of determining      l
l
l
                    valve position or valve location. The licensee's response dated April      l
provided for the plant staff that is involved in these verification
!                    28, 1995, stated that procedure revisions and additional training was      l
activities.
                    provided for the plant staff that is involved in these verification
The ins)ector verified that Operations Management Procedure
                    activities. The ins)ector verified that Operations Management Procedure
2-33. Valve and Breacer Position Verification and Valve Operations, was
                    2-33. Valve and Breacer Position Verification and Valve Operations, was
revised to provide guidance for verifying the position of deenergized
                    revised to provide guidance for verifying the position of deenergized
motor operated valves.
                    motor operated valves. In addition, the licensee provided training to
In addition, the licensee provided training to
,                    establish worker skills in error reduction. The inspector concluded
establish worker skills in error reduction. The inspector concluded
                    that the licensee's corrective actions were appropriate.                   j
,
                                                                                                1
that the licensee's corrective actions were appropriate.
l                                                II. Mainwunce
j
          M1        Conduct of Maintenance
                                                                                                  1
1
1
          M1.1 Unit 2 Outaae Maintenance Items
l
                a. Insoection Scope (62707)
II. Mainwunce
l                   The resident inspector monitored and inspected various work items during     l
M1
l                    the Unit 2 E0C8 refueling outage. Among these were: (1) a modification       :
Conduct of Maintenance
                    to replace the 2A and 2B Emergency Diesel Generator (DG) battery
1
                    chargers: (2) inspection and preventive maintenance on the 2B DG: (3)
M1.1 Unit 2 Outaae Maintenance Items
                    the inspection and reconditioning of valves in the Safety Injection (NI)
a. Insoection Scope (62707)
                    system: (4) the repair of Loose Parts Monitoring System Channel 17.
l
                    Steam Generator (SG) manway: (5) the inspection of the containment sump
The resident inspector monitored and inspected various work items during
                    recirculation valve 2NI-185B: and (6) inspection of the A and D Reactor
l
!                   Coolant Pump (RCP) number 1 seals.       The inspector discussed the
the Unit 2 E0C8 refueling outage.
                                                                                Enclosure 2
Among these were: (1) a modification
to replace the 2A and 2B Emergency Diesel Generator (DG) battery
chargers: (2) inspection and preventive maintenance on the 2B DG: (3)
the inspection and reconditioning of valves in the Safety Injection (NI)
system: (4) the repair of Loose Parts Monitoring System Channel 17.
Steam Generator (SG) manway: (5) the inspection of the containment sump
recirculation valve 2NI-185B: and (6) inspection of the A and D Reactor
!
Coolant Pump (RCP) number 1 seals.
The inspector discussed the
Enclosure 2
i
i
!
!
l
l


    ._   . . ..   _       _     _ _ -   _ . .   _ _ . _         . _ . _ _   _ ___. _ .     .. _
._
                '
.
      .
. ..
                      .
_
                                                          12
_
                      maintenance activities with the licensee, obtained copies of the work
_ _ -
                      packages and observed portions of the maintenance in progress.
_ .
                  b, Observations and Findings
.
                                                                                                    l'
_ _ . _
                      (1)   The Unit 2 125 Volt DC DG battery chargers were replaced under
. _ . _ _
                            station modification CN-21360. The inspector reviewed the work
_ ___. _ .
                            Jackages associated with TN/2/A/1360/00/02E, which governed the A
.. _
                            Xi battery charger replacement., and TN/2/A/1360/00/03E, which
'
                            governed the B DG battery charger replacement. The inspector
.
                            verified that an 8-hour load test on DG chargers- 2A and 28 a
.
                            polarity check, output voltage check and current check were             ,
12
                            successfully completed before the battery chargers were installed.
maintenance activities with the licensee, obtained copies of the work
                            Steel frames and grout pads were fabricated for the chargers. The
packages and observed portions of the maintenance in progress.
                            inspector also verified that provisions for maintaining electrical       i
b, Observations and Findings
                            separation, fabricating and installing electrical enclosures,
l'
                            grounding cables, sealing the cable terminations, and using
(1)
                            crimping tools were included in the work packages.         Cable
The Unit 2 125 Volt DC DG battery chargers were replaced under
                            installation was ')rocedurally controlled, and electrical
station modification CN-21360.
                            isolations and ca]le terminations were recorded in the associated
The inspector reviewed the work
                            procedure. A charger capacity test was satisfactorily performed,
Jackages associated with TN/2/A/1360/00/02E, which governed the A
                            the battery was equalized and charged, batteries were inspected.
Xi battery charger replacement., and TN/2/A/1360/00/03E, which
  .                         and the charger's high and low voltage relay alarms were
governed the B DG battery charger replacement. The inspector
                            calibrated.
verified that an 8-hour load test on DG chargers- 2A and 28 a
                      (2)   The inspection and maintenance plan for the 2B DG included
polarity check, output voltage check and current check were
                            activities typically performed on a five-year interval. The
,
l                           inspector observed portions of the activities in progress and
successfully completed before the battery chargers were installed.
                            reviewed the work package and associated work orders, The
Steel frames and grout pads were fabricated for the chargers. The
                            licensee disassembled sections of the DG: cleaned the engine
inspector also verified that provisions for maintaining electrical
                            block; replaced hoses: refurbished the engine-driven fuel oil
i
                            pump: inspected cams and rollers: inspected the jacket cooling
separation, fabricating and installing electrical enclosures,
                            water pump drive gear: inspected strainers for the starting air
grounding cables, sealing the cable terminations, and using
                            system; and inspected and refurbished a temperature regulating
crimping tools were included in the work packages.
                            valve in the DG jacket cooling water system.
Cable
                      (3)   Multiple check valves, suspected of leaking, were inspected during
installation was ')rocedurally controlled, and electrical
l                           the outage. The licensee inspected valve 2NI-171, Safety
isolations and ca]le terminations were recorded in the associated
,                          Injection pumps to RCS loop C cold leg injection header check
procedure. A charger capacity test was satisfactorily performed,
                            valve, and determined that the valve had low seating contact. A
the battery was equalized and charged, batteries were inspected.
l                           minor modification was generated, and the disc was replaced with a
.
                            new disc of a different design that provided better seating
and the charger's high and low voltage relay alarms were
                            integrity.
calibrated.
                            Valve 2NI-175. RHR header A to RCS Loop C cold leg check valve,
(2)
                            was inspected: the valve was cycled, and the disc operated freely           ,
The inspection and maintenance plan for the 2B DG included
                            without binding. The valve body and disc seats had no indication       H
activities typically performed on a five-year interval. The
                            of degradation. The valve body and disc seats were cleaned, and a           '
l
                            visual inspection revealed wide seat contact.
inspector observed portions of the activities in progress and
,                                                                            Enclosure 2
reviewed the work package and associated work orders,
The
licensee disassembled sections of the DG: cleaned the engine
block; replaced hoses: refurbished the engine-driven fuel oil
pump: inspected cams and rollers: inspected the jacket cooling
water pump drive gear: inspected strainers for the starting air
system; and inspected and refurbished a temperature regulating
valve in the DG jacket cooling water system.
(3)
Multiple check valves, suspected of leaking, were inspected during
l
the outage. The licensee inspected valve 2NI-171, Safety
Injection pumps to RCS loop C cold leg injection header check
,
valve, and determined that the valve had low seating contact.
A
l
minor modification was generated, and the disc was replaced with a
new disc of a different design that provided better seating
integrity.
Valve 2NI-175. RHR header A to RCS Loop C cold leg check valve,
was inspected: the valve was cycled, and the disc operated freely
,
without binding. The valve body and disc seats had no indication
H
of degradation.
The valve body and disc seats were cleaned, and a
'
visual inspection revealed wide seat contact.
Enclosure 2
,
i
i
                                                                                                      ;
:
:
l                                                                                                      l
l


    _     .._ _ . - . _ _ _ . . ._ _ _ _.._ _ _ _ _ _ __.__ _
_
                                                                                                                    :
.._ _ . - . _ _ _ . . ._ _ _ _.._ _ _ _ _ _ __.__ _
                    '
:
        '
'
l                                                                                                                    .
l
                                      ~
'
                                                                                                                    ,
.
                                                                            13
~
                                                                                                                    '
,
                                                Valve 2NI-176 RHR Header A to RCS Looi D cold leg check valve.
13
                                                showed no evidence of seat wear or leacage. The licensee cleaned
Valve 2NI-176 RHR Header A to RCS Looi D cold leg check valve.
                                                the seating surfaces and determined that they were finely. polished
'
                                                                                                                    .
showed no evidence of seat wear or leacage. The licensee cleaned
                                                                                                                    '
the seating surfaces and determined that they were finely. polished
                                                with no indication of degradation.
.'
l                                               The disc in valve 2N!.-169. Safety Injection pumps to RCS lcop D
with no indication of degradation.
l                                              cold leg injection header, was replaced, and the valve body seat
l
l                                               was lapped until good contact could be visually verified. A-small
The disc in valve 2N!.-169. Safety Injection pumps to RCS lcop D
cold leg injection header, was replaced, and the valve body seat
l
l
was lapped until good contact could be visually verified. A-small
!
!
                                                defect was polished out of the valve bonnet. The defect was           i
defect was polished out of the valve bonnet.
                                                believed to have caused minor external leakage in December 1995
The defect was
                                                and had been seal welded at that time to stop the leakage.
i
                                                The inspector did not identify any concerns associated with the NI
believed to have caused minor external leakage in December 1995
                                                system check valve maintenance.
and had been seal welded at that time to stop the leakage.
                                      (4)       Unit 2 Loose Parts Monitoring System Channel 17. SG manway, was
The inspector did not identify any concerns associated with the NI
                                                repaired during a forced outage in December 1996. The channel had
system check valve maintenance.
                                                been declared inoperable on January 2, 1996. Subsequent
(4)
                                                troubleshooting revealed that the failure of the channel
Unit 2 Loose Parts Monitoring System Channel 17. SG manway, was
repaired during a forced outage in December 1996. The channel had
been declared inoperable on January 2, 1996.
Subsequent
troubleshooting revealed that the failure of the channel
originated in the field. The licensee initiated a work request to
,
,
'                                               originated in the field. The licensee initiated a work request to
'
                                                repair the channel during an outage window, at which time the
repair the channel during an outage window, at which time the
                                                necessary containment entry could be made. To notify the NRC that
necessary containment entry could be made. To notify the NRC that
  .
Channel 17 of the Loose Parts Monitoring System was inoperable for
                                                Channel 17 of the Loose Parts Monitoring System was inoperable for
.
.
                                                longer that 30 days, the licensee submitted a s)ecial report on
.
l                                               February 11, 1996, in accordance with Selected .icensee
longer that 30 days, the licensee submitted a s)ecial report on
                                                Commitment Section 16.7-4, and TS 6.9.2.
l
                                                The inspector discussed the repair with licensee personnel,
February 11, 1996, in accordance with Selected .icensee
                                                reviewed the associated work order. WO 96000758-01, and verified     ,
Commitment Section 16.7-4, and TS 6.9.2.
                                                that the channel )roblem had been corrected. The licensee had
The inspector discussed the repair with licensee personnel,
                                                determined that tie acoustic sensor' had an open _ connector at the- :
reviewed the associated work order. WO 96000758-01, and verified
,
that the channel )roblem had been corrected. The licensee had
determined that tie acoustic sensor' had an open _ connector at the-
:
:
                                                female hard line connector point. The sensor was replaced and-
female hard line connector point. The sensor was replaced and-
:
!
satisfactorily tested. The channel was returned to service on
December 16, 1997.
(5)
Prior to the last refueling outage-(2EOC7) the licensee determined
!
that containment sump recirculation valves NI-184A and NI-185B.
l
double-disc gate valves, were susceptible to pressure locking.
!
!
                                                satisfactorily tested. The channel was returned to service on
During 2EOC7 the licensee im)lemented a station modification to
                                                December 16, 1997.
l
                                      (5)      Prior to the last refueling outage-(2EOC7) the licensee determined
install a bonnet vent on eac1 sump recirculation valve.
!                                              that containment sump recirculation valves NI-184A and NI-185B.
The
l                                              double-disc gate valves, were susceptible to pressure locking.
>
!                                              During 2EOC7 the licensee im)lemented a station modification to
,
l     ,
                                                install a bonnet vent on eac1 sump recirculation valve. The         >
1
1
                                                bonnet vents provided a relief path from the valve body to the
bonnet vents provided a relief path from the valve body to the
                                                residual heat removal (RHR) aump discharge line to preclude
residual heat removal (RHR) aump discharge line to preclude
                                                pressurization in the valve Jody and subsequent wedging of the
pressurization in the valve Jody and subsequent wedging of the
i
i
valve discs into their respective seats. The bonnet vent valves
'
'
                                                valve discs into their respective seats. The bonnet vent valves
were intended to remain open during full )ower o)erations,
                                                were intended to remain open during full )ower o)erations,
although they could be. closed to isolate RHR leacage past the
                                                although they could be. closed to isolate RHR leacage past the
containment-side valve disc.
7                                              containment-side valve disc.
7
I                                               During startup from the- previous refueling outage. 2EOC7.- the
I
i
During startup from the- previous refueling outage. 2EOC7.- the
                                                licensee determined that the containment-side seat of 2NI-185A was
i
licensee determined that the containment-side seat of 2NI-185A was
;
;
Enclosure 2
.
.
                                                                                                  Enclosure 2
l
l
\
\\
                                                                                                        .
.
i                                 .                                   -.           -           -
i
                                                                                                      .
.
-.
-
-
.


  . . _. _ ._._. .. _           _ _ . _ . . _ _                 _ _ . . . . _ _ _ _ _ _ _ . _ _
. . _. _ ._._. .. _
                                                                                                                ,
_ _ . _ . . _ _
                    -
_ _ . . . . _ _ _ _ _ _ _ . _ _
                                                                                                              I
,
          .
I
                                                                                                                i
i
                          .
-
l                                                                 14                                           i
.
                                                                                                                >
.
                              leaking.           Since the bonnet vent valve (2NI-488) bypassed the RHR       :
l
i                             suction-side disc a minor flow 3ath was created from the FWST.                   !
14
L                             via the RHR suction header. to t1e containment sump. To block the               !
i
l                             leakage, vent valve 2NI-488 was locked closed. A work order was                 i
>
;                             generated to inspect and repair 2NI-185B during 2E0C8.                           ;
leaking.
l                             The licensee opened the valve to inspect the seatirig surfaces                   l
Since the bonnet vent valve (2NI-488) bypassed the RHR
                              during the refueling outage: the inspection results were
:
                                                                                                                ~
i
suction-side disc a minor flow 3ath was created from the FWST.
L
via the RHR suction header. to t1e containment sump.
To block the
!
l
leakage, vent valve 2NI-488 was locked closed. A work order was
i
;
generated to inspect and repair 2NI-185B during 2E0C8.
;
l
The licensee opened the valve to inspect the seatirig surfaces
l
l
during the refueling outage: the inspection results were
~
documented in PIP 2-C97-1066. At several locations around the
perimeter of the containment-side valve body seat, small
'
l
l
                              documented in PIP 2-C97-1066. At several locations around the                    '
semicircular indicat ons were visible. The containment-side disc
                              perimeter of the containment-side valve body seat, small
i
l                              semicircular indicat ions were visible. The containment-side disc
l-
l-                             seat had similar marks where the two surfaces had mated. The                     i
seat had similar marks where the two surfaces had mated. The
                              licensee could not determine why the pattern was present on the                 '
i
l                             valve body seat, nor coula the valve vendor explain these                       !
licensee could not determine why the pattern was present on the
;                             indications. The indications in the seat surfaces were the likely               !
'
!                             cause of the seat leakage during the previous operating cycle.
l
                                                                                                                )
valve body seat, nor coula the valve vendor explain these
!
;
indications. The indications in the seat surfaces were the likely
!
!
cause of the seat leakage during the previous operating cycle.
)
l
l
The licensee opted to leave the valve in its as found condition to
!
'
'
                              The licensee opted to leave the valve in its as found condition to              !
avoid disturbing the seating of the RHR-side disc. The inspector
                              avoid disturbing the seating of the RHR-side disc. The inspector                 i
i
questioned this decision, since they had been aware of the seat
:
,
,
'
'
                              questioned this decision, since they had been aware of the seat                  :
leakage during the preceding operating cycle and had ample time to
                              leakage during the preceding operating cycle and had ample time to               ,
l
l                             plan for re) air during the refueling outage. The licensee                       !
plan for re) air during the refueling outage.
l.                             explained tlat extensive time and resources could be allocated to               i
The licensee
l                             improve the containment-side di.;c seating, but that improvement
,
j.                             could not be guaranteed and that the RHR-side disc seating                       '
!
;                             integrity could be disturbed in the process.                                     i
l.
                              To test valve seating integrity.of the containment-side disc. the               <
explained tlat extensive time and resources could be allocated to
                              licensee applied 50 psig from the RHR pump side of the valve with
i
l                             vent valve 2NI-488 closed: no signs of leakage into the                         ,
l
improve the containment-side di.;c seating, but that improvement
j.
could not be guaranteed and that the RHR-side disc seating
'
;
integrity could be disturbed in the process.
i
To test valve seating integrity.of the containment-side disc. the
<
licensee applied 50 psig from the RHR pump side of the valve with
l
vent valve 2NI-488 closed: no signs of leakage into the
,
'
'
                              containment sump were identified. Valve 2NI-488 was then' opened.               !
containment sump were identified.
!                             and leakage into the sump was observed. Valve DI-488 was then
Valve 2NI-488 was then' opened.
:                             closed, and leakage into the sump was isolated oy the seating
!
l                             integrity of the RHR-side disc and the bonnet vent valve. An                     i
!
                              operability evaluation, documented in PIP 2-C97-1172. stated that
and leakage into the sump was observed.
                              (1) valve 2NI-488 will be administratively controlled in the-                     l
Valve DI-488 was then
                              closed position, and (2) valve 2NI-185A is operable with 2NI-488
:
,                              closed. The inspector concluded that the o)erability evaluation
closed, and leakage into the sump was isolated oy the seating
i                             and actions taken to address seat leakage w1ile accounting for
l
!                             pressure locking and thermal binding were appropriate.
integrity of the RHR-side disc and the bonnet vent valve. An
                        (6)   The inspector observed RCP seal inspections and maintenance. The
i
!                             ins)ector also reviewed the task completian comments associated
operability evaluation, documented in PIP 2-C97-1172. stated that
                              wit 1 work orders 96098973-01 and 96098974-01 (for 2A and 2D RCP
(1) valve 2NI-488 will be administratively controlled in the-
                              seal work, respectively). The 2D RCP numoer 1 seal was cleaned
closed position, and (2) valve 2NI-185A is operable with 2NI-488
                              and inspected verified to be in good condition. and reinstalled.
closed.
,                              A chip was found in the outer edge of the 2A 'RCP number 1 seal
The inspector concluded that the o)erability evaluation
,
i
and actions taken to address seat leakage w1ile accounting for
!
pressure locking and thermal binding were appropriate.
(6)
The inspector observed RCP seal inspections and maintenance. The
!
ins)ector also reviewed the task completian comments associated
wit 1 work orders 96098973-01 and 96098974-01 (for 2A and 2D RCP
seal work, respectively). The 2D RCP numoer 1 seal was cleaned
and inspected verified to be in good condition. and reinstalled.
A chip was found in the outer edge of the 2A 'RCP number 1 seal
,
surface. A new set of stationary and running seals was installed,
'
'
                              surface. A new set of stationary and running seals was installed,
j
j                              and the maintenance personnel verified that the seal moved freely
and the maintenance personnel verified that the seal moved freely
j                             up and down.
j
up and down.
'
'
                                                                                                  Enclosure 2
Enclosure 2
i
i
                                                                                                                i
i
                                                                                                                  i
i
                                                                                                                !
l
                                                                                                                !
..
                                                                                                                  l
.
l            ..       .     -                               -
-
-
.


    .   .                             .     .-   --- -             -     ..   .   . - .   .
.
          *
.
      .
.
.-
--- -
-
..
.
. - .
.
*
.
i
i
                    .
.
                                                      15
15
                        The inspector noted that RCP seal work was conducted in confined
The inspector noted that RCP seal work was conducted in confined
                        areas around the RCPs. The work areas were difficult to access
areas around the RCPs.
                        and cramped.   In addition, cleanliness and lighting levels during
The work areas were difficult to access
                        the maintenance activities were adversely affected by the cramped
and cramped.
                        working spaces.
In addition, cleanliness and lighting levels during
              c. Conclusions
the maintenance activities were adversely affected by the cramped
                  The inspector concluded that, in general, outage-related maintenance       '
working spaces.
                  activities were ap]ropriately conducted. Although multiple barriers to
c. Conclusions
                  minimizing the risc of human error during RCP seal maintenance were
The inspector concluded that, in general, outage-related maintenance
                  noted, the ins)ector was unaware of any human performance problems
'
                  associated wit 1 the work.
activities were ap]ropriately conducted.
            M1.2 Unit 2 Nuclear Service Water Pumo Motor Reolacement
Although multiple barriers to
              a. Insoection Scope (62707)
minimizing the risc of human error during RCP seal maintenance were
                  The inspector reviewed the licensee's resolution to elevated vibration
noted, the ins)ector was unaware of any human performance problems
                  levels associated with the 2B nuclear service water pump / motor assembly.
associated wit 1 the work.
                  The 2B nuclear service water pump has experienced intermittent periods
M1.2 Unit 2 Nuclear Service Water Pumo Motor Reolacement
                  of elevated vibration since 1994. During the inspection period, the
a. Insoection Scope (62707)
  .              licensee identified problems with the condition of the s
The inspector reviewed the licensee's resolution to elevated vibration
                  service water replacement motor stored in the warehouse.Accordingly,
levels associated with the 2B nuclear service water pump / motor assembly.
                                                                                pare nuclear
The 2B nuclear service water pump has experienced intermittent periods
                  the inspector reviewed the results of previous licensee assessments of
of elevated vibration since 1994.
                  spare motor storage practices, previous motor failures, and an ongoing
During the inspection period, the
                  licensee assessment of maintenance and storage practices for spare
licensee identified problems with the condition of the s
                  motors.
service water replacement motor stored in the warehouse. pare nuclear
              b. Observations and Findinas
.
                  The 28 Nuclear Service Water pump is a smooth running pump with normally
Accordingly,
                  low measured vibration levels. In 1994 and 1995 the pump / motor assembly
the inspector reviewed the results of previous licensee assessments of
                  3eriodically experienced an increase in vibration relative to its past
spare motor storage practices, previous motor failures, and an ongoing
                  )aseline performance and also relative to the other nuclear service
licensee assessment of maintenance and storage practices for spare
                  water pumps. The relative increase in vibration levels caused the pump
motors.
                  to enter Alert levels although it continued to remain in the smooth
b. Observations and Findinas
                  running range, As a result of this experience, the licensee performed
The 28 Nuclear Service Water pump is a smooth running pump with normally
                  extensive inspection of this pump and motor during the current refueling
low measured vibration levels.
                  outage. Internal inspection of the pump showed no damage or
In 1994 and 1995 the pump / motor assembly
                  degradation. Vibration measurements made during an uncoupled run of the
3eriodically experienced an increase in vibration relative to its past
                  motor indicated that the source of elevated vibrations was confined to
)aseline performance and also relative to the other nuclear service
                  the motor. Based on additional analysis of vibration dr.ta performed by         '
water pumps. The relative increase in vibration levels caused the pump
                  Electrical System Support (ESS) personnel, the licensee determined that
to enter Alert levels although it continued to remain in the smooth
                  an internal rub was occurring in the motor and elected to replace it.
running range,
                  The spare nuclear service water pump motor developed severe oil leaks
As a result of this experience, the licensee performed
extensive inspection of this pump and motor during the current refueling
outage.
Internal inspection of the pump showed no damage or
degradation.
Vibration measurements made during an uncoupled run of the
motor indicated that the source of elevated vibrations was confined to
the motor. Based on additional analysis of vibration dr.ta performed by
'
Electrical System Support (ESS) personnel, the licensee determined that
an internal rub was occurring in the motor and elected to replace it.
The spare nuclear service water pump motor developed severe oil leaks
from its lower bearing during initial check out runs performed in the
'
'
                  from its lower bearing during initial check out runs performed in the
motor test shop prior to its installation.
                  motor test shop prior to its installation.     Inspections of the saare
Inspections of the saare
                  motor internals performed by an offsite vendor determined that tie lower
motor internals performed by an offsite vendor determined that tie lower
                                                                          Enclosure 2
Enclosure 2
:
:
I
I


                                                .     __       , -.   -.
.
      *
__
    .
,
                _
-.
                                                  16
-.
              bearing surfaces were partially melted due to rubbing or inadequate
*
              lubrication. Additional testing revealed more problems and the spare
.
              motor was considered unacceptable for use and required extensive rework
_
              and repair. The licensee subsequently performed internal inspections of   l
16
              the installed nuclear service water pump motor and determined the cause   I
bearing surfaces were partially melted due to rubbing or inadequate
              of the eleyated vibration resulted from mechanical looseness in the       ,
lubrication.
              upper bearing components. An off center condition in the lower bearing   1
Additional testing revealed more problems and the spare
              housing was also discovered. The licensee corrected these                 '
motor was considered unacceptable for use and required extensive rework
              adeficiencies, which eliminated the elevated vibration characteristic as i
and repair.
              measured in uncoupled runs and coupled inservice pump tests.               l
The licensee subsequently performed internal inspections of
                In 1996, a residual heat removal pump motor failed soon after functional
the installed nuclear service water pump motor and determined the cause
              testing. The licensee determined that poor storage conditions may have
of the eleyated vibration resulted from mechanical looseness in the
              contributed to this failure (refer to NRC Inspection Report 96-13). The
,
              licensee has recently performed two assessments of motor storage and     I
upper bearing components. An off center condition in the lower bearing
              handling practices and identified several findings and recommendations.   I
housing was also discovered.
              Inspector Followup Item (IFI) 50-413.414/97-07-03, Review Corrective
The licensee corrected these
              Actions For Storage and Handling Assessment Findings, is identified to
adeficiencies, which eliminated the elevated vibration characteristic as
              verify that the licensee has completed corrective actions resulting from
measured in uncoupled runs and coupled inservice pump tests.
              the followirig assessments: (1) Assessment Report CTS-09-96. Electric     i
In 1996, a residual heat removal pump motor failed soon after functional
              Motor P.M. - 12/2/96; and (2) Assessment Report SA-97-61(CN)(SRG),         j
testing. The licensee determined that poor storage conditions may have
              Assessment of Warehouse Material Condition - 4/23-28/97.
contributed to this failure (refer to NRC Inspection Report 96-13). The
  .
licensee has recently performed two assessments of motor storage and
          c. Conclusions
handling practices and identified several findings and recommendations.
              The licensee's resolution of long-standing elevated vibration levels       ,
Inspector Followup Item (IFI) 50-413.414/97-07-03, Review Corrective
              associated with the Unit 2B nuclear service water pump motor was very     !
Actions For Storage and Handling Assessment Findings, is identified to
              good. Deficiencies identified with a spare nuclear service water pump
verify that the licensee has completed corrective actions resulting from
              motor, a previous motor failure, and findings identified by licensee
the followirig assessments:
              assessment of warehouse storage and handling 3ractices raised questions
(1) Assessment Report CTS-09-96. Electric
              about control and storage of spare motors. T1e issue is identified as
Motor P.M. - 12/2/96; and (2) Assessment Report SA-97-61(CN)(SRG),
              an Inspector Followup Item and will be reviewed during a future
j
              inspection.
Assessment of Warehouse Material Condition - 4/23-28/97.
                                                                                        1
.
        M2    Maintenance and Material Condition of Facilities and Equipment
c. Conclusions
        M2.1 Observation of Unit 2 Inservice Insoection Work Activities
The licensee's resolution of long-standing elevated vibration levels
          a. Insoection Scope (73753)
,
              The present Unit 2 E0C8 refueling outage was the first outage, of the
associated with the Unit 2B nuclear service water pump motor was very
              first inspection period, of the second inservice inspection interval.
good.
              The applicable code for Unit 2, for the second inservice inspection
Deficiencies identified with a spare nuclear service water pump
              interval was the American Society of Mechanical Engineers (ASME) Code
motor, a previous motor failure, and findings identified by licensee
l            Section XI, 1989 Edition, no Addenda. The inspector reviewed
assessment of warehouse storage and handling 3ractices raised questions
l            documentation and observed ultrasonic, magnetic ) article, and liquid
about control and storage of spare motors. T1e issue is identified as
an Inspector Followup Item and will be reviewed during a future
inspection.
M2
Maintenance and Material Condition of Facilities and Equipment
M2.1 Observation of Unit 2 Inservice Insoection Work Activities
a. Insoection Scope (73753)
The present Unit 2 E0C8 refueling outage was the first outage, of the
first inspection period, of the second inservice inspection interval.
The applicable code for Unit 2, for the second inservice inspection
interval was the American Society of Mechanical Engineers (ASME) Code
l
l
Section XI, 1989 Edition, no Addenda. The inspector reviewed
l
documentation and observed ultrasonic, magnetic ) article, and liquid
l
penetrant examination activities to determined w1 ether the inservice
~
~
              penetrant examination activities to determined w1 ether the inservice
inspection (ISI) activities were performed in accordance with Technical
              inspection (ISI) activities were performed in accordance with Technical
specifications (TS), the applicable ASME Code, and/or requirements
              specifications (TS), the applicable ASME Code, and/or requirements
imposed by NRC/ industry initiatives.
              imposed by NRC/ industry initiatives.
'
'
                                                                        Enclosure 2
Enclosure 2
l
l


                                                                                      1
1
      *
*
    .
.
                                              17
17
        b. Observations and Findinos
b. Observations and Findinos
            The inspector reviewed the ISI outage examination plan and certification
The inspector reviewed the ISI outage examination plan and certification
            records for all NDE examiners aerforming ISI examinations this outage.
records for all NDE examiners aerforming ISI examinations this outage.
l           The following procedures, whic1 were used in the examination activities
l
            observed by the inspector, were reviewed for technical content:
The following procedures, whic1 were used in the examination activities
            *      NDE-600. " Ultrasonic Examination of Similar Metal Welds in Wrought l
observed by the inspector, were reviewed for technical content:
                  Ferritic and Austenitic Piping." Revision 9
NDE-600. " Ultrasonic Examination of Similar Metal Welds in Wrought
            .
*
                  NDE-610. " Ultrasonic Examination of Dissimilar Metal Welds and
Ferritic and Austenitic Piping." Revision 9
                  Cast Austenitic Welds Using Refracted Longitudinal and Shear       i
NDE-610. " Ultrasonic Examination of Dissimilar Metal Welds and
                  Waves." Revision 4
.
            .
Cast Austenitic Welds Using Refracted Longitudinal and Shear
                  NDE-660 " Ultrasonic Examination of Reactor Pressure Vessel Head
i
                  to Flange Welds." Revision 2
Waves." Revision 4
            .      NDE-25. " Magnetic Particle Examination." Revision 17
NDE-660 " Ultrasonic Examination of Reactor Pressure Vessel Head
            .     NDE-35. " Liquid Penetrant Examination." Revision 16
.
            Examinations of the following components were also observed by the
to Flange Welds." Revision 2
  .        inspector to determine if the examination procedures were followed,
NDE-25. " Magnetic Particle Examination." Revision 17
            whether examination personnel were knowledgeable of the examination
.
            method and operation of the test equipment, and if the examination
NDE-35. " Liquid Penetrant Examination." Revision 16
            results and evaluation of the results were recorded as specified in the
.
            ISI program and NDE procedures.
Examinations of the following components were also observed by the
          . Welds Examined                       NDE Method Used
inspector to determine if the examination procedures were followed,
            2RPV-101-101***                       Ultrasonic Examination
.
            2RPV-102-101***                       Ultrasonic Examination
whether examination personnel were knowledgeable of the examination
            2CA-59-8                             Ultrasonic Examination
method and operation of the test equipment, and if the examination
            2CA-59-11                           Ultrasonic Examination
results and evaluation of the results were recorded as specified in the
            2RPV-101-101                         Magnetic Particle Examination         i
ISI program and NDE procedures.
            2CA-59-8                             Magnetic Particle Examination         i
. Welds Examined
            2CA-59-11                           Magnetic Particle Examination
NDE Method Used
            2NV-242-3                           Liquid Penetrant Examination
2RPV-101-101***
            2NV-242-4                             Liquid Penetrant Examination
Ultrasonic Examination
            2NV-242-10                           Liquid Penetrant Examination         1
2RPV-102-101***
            2NV-242-11                           Liquid Penetrant Examination         l
Ultrasonic Examination
            2RPV-W80-101SE                       Liquid Penetrant Examination         i
2CA-59-8
            2RPV-W81-101SE                       Liquid Penetrant Examination
Ultrasonic Examination
            2RPV-W82-101SE                       Liquid Penetrant Examination
2CA-59-11
            2RPV-W79-101SE                       Liquid Penetrant Examination
Ultrasonic Examination
            2RPV-W80-101                         Liquid Penetrant Examination
2RPV-101-101
,           2RPV-W81-101                         Liquid Penetrant Examination
Magnetic Particle Examination
l           2RPV-W82-101                         Liquid Penetrant Examination
2CA-59-8
l           2RPV-W79-101                         Liquid Penetrant Examination
Magnetic Particle Examination
2CA-59-11
Magnetic Particle Examination
2NV-242-3
Liquid Penetrant Examination
2NV-242-4
Liquid Penetrant Examination
2NV-242-10
Liquid Penetrant Examination
2NV-242-11
Liquid Penetrant Examination
2RPV-W80-101SE
Liquid Penetrant Examination
i
2RPV-W81-101SE
Liquid Penetrant Examination
2RPV-W82-101SE
Liquid Penetrant Examination
2RPV-W79-101SE
Liquid Penetrant Examination
2RPV-W80-101
Liquid Penetrant Examination
,
2RPV-W81-101
Liquid Penetrant Examination
l
2RPV-W82-101
Liquid Penetrant Examination
l
2RPV-W79-101
Liquid Penetrant Examination
!
!
!                                                                   Enclosure 2
!
Enclosure 2


        _         _   .               __       _     _-.     _   _   ..         . _ . .
_
    .
_
.
__
_
_-.
_
_
..
. _ .
.
.
,
,
  ,
,
,
                .
                                                  18
              **** Note: Only portions of the 0 degree and 45 degree scans for these      !
,
,
              reactor vessel head welds were observed due to radiation dose             >
.
              limitations.
18
**** Note: Only portions of the 0 degree and 45 degree scans for these
!
reactor vessel head welds were observed due to radiation dose
,
>
'
'
                                                                                          I
limitations.
                                                                                          l
I
          c. Conclusion
c. Conclusion
              NDE personnel certifications records, weld examinations, and NDE
NDE personnel certifications records, weld examinations, and NDE
              examination procedures were in accordance with Code requirements.
examination procedures were in accordance with Code requirements.
      M2.2 Observation of Unit 2 Steam Generator Eddy Current Data Acouisition
M2.2 Observation of Unit 2 Steam Generator Eddy Current Data Acouisition
              Activities
Activities
          a. Insoection Scooe (73753)
a. Insoection Scooe (73753)
              The inspector reviewed documentation and observed eddy current data         ,
The inspector reviewed documentation and observed eddy current data
l             acquisition activities to dstermine whether these activities were           i
l
              performed in accordance with Technical Specifications (TS), the 1989       j
acquisition activities to dstermine whether these activities were
              Edition of Section XI to the ASME Code, and requirements imposed by         -
,
              NRC/ industry initiatives.                                                   ,
i
                                                                                          ;
performed in accordance with Technical Specifications (TS), the 1989
j
Edition of Section XI to the ASME Code, and requirements imposed by
-
NRC/ industry initiatives.
,
;
;
          b. Observations and Findinas
b. Observations and Findinas
,
,
                                                                                          i
i
l.           The licensee was performing bobbin coil eddy current examinations of 62%   !
l.
              of the tubes in all four steam generators for Unit 2. In addition, a       i
The licensee was performing bobbin coil eddy current examinations of 62%
              25% sample of the hot leg tube sheet transitions in each steam generator   '
of the tubes in all four steam generators for Unit 2.
              will be examined using a motor rotating pancake coil (MRPC). At the
In addition, a
              time of this ins)ection the licensee had just started the examination
25% sample of the hot leg tube sheet transitions in each steam generator
;            activities and t1e data acquired was being sent directly to the McGuire
'
will be examined using a motor rotating pancake coil (MRPC). At the
time of this ins)ection the licensee had just started the examination
activities and t1e data acquired was being sent directly to the McGuire
;
Nuclear Plant for analysis.
Therefore, the inspector's examination of
'
'
              Nuclear Plant for analysis. Therefore, the inspector's examination of
l
l
these activities was limited to review of the outage eddy current
'
'
              these activities was limited to review of the outage eddy current
inspection plan, examiner and equipment certifications, and review of
              inspection plan, examiner and equipment certifications, and review of
examination procedures No. NDE-707 Revision 3, "Multifrequency Eddy
l
l
              examination procedures No. NDE-707 Revision 3, "Multifrequency Eddy
Current Examination of Non-Ferrous Tubing. Sleeves and Plugs Using a
              Current Examination of Non-Ferrous Tubing. Sleeves and Plugs Using a
Motorized Rotating Coil Probe", and No. NDE-701 Revision 3.
              Motorized Rotating Coil Probe", and No. NDE-701 Revision 3.
"Multifrequency Eddy Current Examination of Steam Generator Tubing at
              "Multifrequency Eddy Current Examination of Steam Generator Tubing at
McGuire. Catawba and Oconee Nuclear Stations and observation of the eddy
              McGuire. Catawba and Oconee Nuclear Stations and observation of the eddy
.
.
current data acquisition process,
i
i
              current data acquisition process,
l-
l-       c. Conclusion
c. Conclusion
              Review of the eddy current outage plan, equipment setup and acquisition
Review of the eddy current outage plan, equipment setup and acquisition
              procedures, personnel and equipment certifications, and observation of
procedures, personnel and equipment certifications, and observation of
l           data acquisition activities revealed that required documentation was
l
l             available and complete. and data acquisition personnel were
data acquisition activities revealed that required documentation was
l             knowledgeable of the eddy current examination process.
l
available and complete. and data acquisition personnel were
l
knowledgeable of the eddy current examination process.
l
l
!
!
4
4
U
U
.
Enclosure 2
                                                                      Enclosure 2
.
i
i
l
l
l
l


      '
    e
                                                  19
        M2.3 Unit 2 Flow Accelerated Corrosion (FAC) Proaram                            l
          a. Insoection Scooe (49001)                                                    !
                                                                                        l
              The inspector held discussions with the licensee's erosion / corrosion    !
              engineers to determine the scope of FAC examinations scheduled for this
              outage: the condition of the plant piping as revealed by inspection: the
              extent of pipe replacement recuired: and whether proper examination
              expansion was performed when cefective components were found.
          b. Observations and Findinas
                                                                                        i
              The licensee's FAC program for Unit 2 was based on the Electric Power
              Research Institute's (EPRI) Document No. NSAC-202L. " Recommendation for
              an Effective Flow Accelerated Corrosion Program." Revision 1. In          ,
              addition. EPRI's CHEC Works Computer Codes were used, as well as          '
              portions of the licensee's prev'ous program for erosion / corrosion to
              identify components which will require examination. Initially, a sample
              of 55 components were scheduled for ultrasonic examination during the
              EOC-8 refueling outage. The sample also included the entire component.
              upstream and downstream of the initial component. The licensee planned    !
              to replace six components without further examination, based on            '
  .
              corrosion growth rates confirmed last outage. The examination of
              components for FAC this outage were approximately 40% complete when
              audited by the inspector. As a result of these examinations, five
              additional components will be replaced this outage. The inspector
              verified that expansion ins)ections.were correctly performed as a result
              of the components found to 3e unacceptable based on inspections
              performed this outage. The inspector also inquired as to why the
              initial inspection sample was so small. The licensee stated that
              smaller samples with a high volume of essential components. based on
              tracking and trending was now possible on Unit 2 for the following
              reasons:
              .      Significant previous replacements of components with
                      erosion / corrosion resistant materials.
              .      Changes in secondary chemistry control have reduced wear rates
                      significantly.
              .      The entire upstream and downstream components from a sample
'
'
                      selected for inspection are also examined.
e
              .      Unit 2 was designed with heater drains and moisturizer separator
19
                      reheater drains which have erosion / corrosion resistant materials
M2.3 Unit 2 Flow Accelerated Corrosion (FAC) Proaram
                      downstream of all control valves.
a. Insoection Scooe (49001)
              .      FAC program maturity.
The inspector held discussions with the licensee's erosion / corrosion
            The inspector agreed with the licensee's reasoning.
!
,                                                                      Enclosure 2
engineers to determine the scope of FAC examinations scheduled for this
outage: the condition of the plant piping as revealed by inspection: the
extent of pipe replacement recuired: and whether proper examination
expansion was performed when cefective components were found.
b. Observations and Findinas
i
The licensee's FAC program for Unit 2 was based on the Electric Power
Research Institute's (EPRI) Document No. NSAC-202L. " Recommendation for
an Effective Flow Accelerated Corrosion Program." Revision 1.
In
addition. EPRI's CHEC Works Computer Codes were used, as well as
,
'
portions of the licensee's prev'ous program for erosion / corrosion to
identify components which will require examination.
Initially, a sample
of 55 components were scheduled for ultrasonic examination during the
EOC-8 refueling outage.
The sample also included the entire component.
upstream and downstream of the initial component. The licensee planned
to replace six components without further examination, based on
'
corrosion growth rates confirmed last outage.
The examination of
.
components for FAC this outage were approximately 40% complete when
audited by the inspector. As a result of these examinations, five
additional components will be replaced this outage.
The inspector
verified that expansion ins)ections.were correctly performed as a result
of the components found to 3e unacceptable based on inspections
performed this outage.
The inspector also inquired as to why the
initial inspection sample was so small.
The licensee stated that
smaller samples with a high volume of essential components. based on
tracking and trending was now possible on Unit 2 for the following
reasons:
Significant previous replacements of components with
.
erosion / corrosion resistant materials.
Changes in secondary chemistry control have reduced wear rates
.
significantly.
The entire upstream and downstream components from a sample
.
selected for inspection are also examined.
'
Unit 2 was designed with heater drains and moisturizer separator
.
reheater drains which have erosion / corrosion resistant materials
downstream of all control valves.
FAC program maturity.
.
The inspector agreed with the licensee's reasoning.
Enclosure 2
,
:
:
!
!
l
l


  .                                               .                   - . _ .             _
.
.
- . _ .
_
l
l
l
l
    .
.
                  .
.
                                                    20                                     I
20
                                                                                            i
I
            c. Conclusion
c. Conclusion
                                                                                            ,
,
                The licensee has implemented an effective program for the detection of       )
The licensee has implemented an effective program for the detection of
)
l
l
flow accelerated corrosion in components.
This program was based on
'
'
recommendations found in recognized industry standards.
M7
Quality Assurance In Maintenance Activities
.
l
M7.1 Maintenance Self Assessment Prooram
a. Insoection Scone (62707. 40500)
The inspector reviewed the status of maintenance and work control self-
assessment programs.
The inspection included review of NSD 607. Self-
Assessments; maintenance and work control annual assessment plans for
1996 and 1997: selected self-assessment reports; and maintenance / work
l
control performance indicators,
b
Observations and Findinas
The licensee's self-assessment program consisted of two types of self-
assessments, routine and non-routine.
Routine assessments were
'.
performed on a quarterly or semi-annual basis and included topics such
j
as PIPS, Job Observations. Rework. Material Condition / Housekeeping. Work
Order Quality. Budget. Radiation Dose / Contamination. Planning, and Work
Control Process.
Non-routine assessments were performed when the need
i
was apparent to management to assess a certain area or function. Some
1
examples were Procedure Use and Adherence. Environmental Compliance.
Pre-job Briefings. Control of Vendors, and Work Task Skills.
Corrective
actions from the self-assessments were tracked for completion through
PIPS.
The inspector noted that the self-assessments that were reviewed
effectively identified areas for improvement, and appropriate corrective
'
actions were recommended and entered in the Problem Investigation
'
'
                flow accelerated corrosion in components. This program was based on        '
Process for resolution.
                recommendations found in recognized industry standards.                    !
Of the routine assessments reviewed the
      M7      Quality Assurance In Maintenance Activities      .
inspector considered the quarterly assessment of Job Observation Trends,
l      M7.1 Maintenance Self Assessment Prooram
initiated in 1997, to be an effective use of the data generated by first
            a. Insoection Scone (62707. 40500)
line supervisor observations.
                The inspector reviewed the status of maintenance and work control self-
Since the initiation of the Maintenance / Work Control Self-Assessment
                assessment programs. The inspection included review of NSD 607. Self-
Programs in mid and late 1995. performance indicators such as work order
                Assessments; maintenance and work control annual assessment plans for        i
backlog, schedule efficiency, and control board indication problems all
                1996 and 1997: selected self-assessment reports; and maintenance / work    l
showed improving trends.
                control performance indicators,
c.
          b    Observations and Findinas
Conclusion
                The licensee's self-assessment program consisted of two types of self-      l
                assessments, routine and non-routine.    Routine assessments were
'.              performed on a quarterly or semi-annual basis and included topics such      j
                as PIPS, Job Observations. Rework. Material Condition / Housekeeping. Work
                Order Quality. Budget. Radiation Dose / Contamination. Planning, and Work
                Control Process. Non-routine assessments were performed when the need        i
                was apparent to management to assess a certain area or function. Some        1
                examples were Procedure Use and Adherence. Environmental Compliance.
                Pre-job Briefings. Control of Vendors, and Work Task Skills. Corrective
                actions from the self-assessments were tracked for completion through
                PIPS.
                The inspector noted that the self-assessments that were reviewed            !
                effectively identified areas for improvement, and appropriate corrective    '
                actions were recommended and entered in the Problem Investigation            '
                Process for resolution. Of the routine assessments reviewed the
                inspector considered the quarterly assessment of Job Observation Trends,
                initiated in 1997, to be an effective use of the data generated by first
                line supervisor observations.
                Since the initiation of the Maintenance / Work Control Self-Assessment
                Programs in mid and late 1995. performance indicators such as work order
                backlog, schedule efficiency, and control board indication problems all
                showed improving trends.
        c.     Conclusion                                                                   ;
'
'
                Based on the inspection described above. the inspector concluded that
Based on the inspection described above. the inspector concluded that
                the maintenance / work control self-assessment programs effectively
the maintenance / work control self-assessment programs effectively
identified areas for improvement and appropriate corrective actions.
i
i
                identified areas for improvement and appropriate corrective actions.
Enclosure 2
                                                                              Enclosure 2   4
4
'
'
                                                                                            l


  . - -       . __       _...     . _ . _ . . . . _ _ . _ . _ _ . . _                   _ _ . _ . - . . _ . _ _ _ . _ . . _ . _
. - -
                                c'                                                                                                           l
. __
                *
_...
l          .
. _ . _ . . . . _ _ . _ . _ _ . . _
                              .
_ _ . _ . - . . _ . _ _ _ . _ . . _ . _
                                                                                21                                                           ,
c'
                                                                                                                                              1
l
                            The self-assessments apparently contributed to improvemert. in the
l
                            performance of the Maintenance and Work Control organizations.
*
                                                                        III. Enaineering
.
.
21
,
The self-assessments apparently contributed to improvemert. in the
performance of the Maintenance and Work Control organizations.
III. Enaineering
I
I
'
'
                    El     Conduct of Engineering
El
                    El.1 Unit 2 Control Rod Tio Crackina
Conduct of Engineering
El.1 Unit 2 Control Rod Tio Crackina
l
l
;
;
                      a. Insoection Scoce (61726. 37551)
a. Insoection Scoce (61726. 37551)
                            During routine outage related examinations of Unit 2 control rod .
During routine outage related examinations of Unit 2 control rod .
assemblies, the licensee identified a higher than expected number of
,
,
                            assemblies, the licensee identified a higher than expected number of
!
!                          control rods with tip cracking. The inspector reviewed the licensee's
control rods with tip cracking. The inspector reviewed the licensee's
L                           testing procedure, results of the examinations, and corrective actions
L
;_                         for test failures,
testing procedure, results of the examinations, and corrective actions
                      b. Observations and Findinos
;_
l                          Industry experience has shown that control rods develop tip cracking as
for test failures,
!                          a result of cladding interaction caused by swelling of the absorber
b. Observations and Findinos
l
l
                            material inside this portion of the rods. . Tip cracking and other
Industry experience has shown that control rods develop tip cracking as
  .
!
                            potential control rod defects such as mechanical wearing are monitored
a result of cladding interaction caused by swelling of the absorber
                            every refueling outage by the licensee using procedure PT/0/A/4150/26.
l
                            Rod Control Cluster Assembly (RCCA) Ultrasonic / Eddy Current Testing.                                             ,
material inside this portion of the rods. . Tip cracking and other
                            The inspector. discussed the results of the testing with reactor                                                   '
potential control rod defects such as mechanical wearing are monitored
                            engineering personnel. The inspector observed that twenty.six control
.
                            rod assemblies were found with indications of tip cracking. This
every refueling outage by the licensee using procedure PT/0/A/4150/26.
            -
Rod Control Cluster Assembly (RCCA) Ultrasonic / Eddy Current Testing.
                            exceeded the expected number of twelve control rod assemblies aredicted                                           ,
,
                            to have tip cracks The licensee ordered additional rod assem) lies                                               '
The inspector. discussed the results of the testing with reactor
                            fabricated by the vendor and replaced each control rod assembly that had-
'
                            evidence of tip cracking. The inspector verified by reviewing control
engineering personnel.
                            rod assembly deficiency evaluations that the twenty six assemblies were
The inspector observed that twenty.six control
                            replaced.                                                                                                         '
rod assemblies were found with indications of tip cracking.
                      c. Conclusions
This
                            The licensee's actions to replace all control rod assemblies that had
exceeded the expected number of twelve control rod assemblies aredicted
                            evidence of tip cracking were appropriate.
-
                    E2     Engineering Support of Facilities and Equipment
,
                    E2.1 Review of Tentative Repair Activities for the Manway Cover on the Unit 2
to have tip cracks
                            Pressurizer
The licensee ordered additional rod assem) lies
                      a. Insoection Scone (62001)
'
fabricated by the vendor and replaced each control rod assembly that had-
evidence of tip cracking.
The inspector verified by reviewing control
rod assembly deficiency evaluations that the twenty six assemblies were
replaced.
'
c. Conclusions
The licensee's actions to replace all control rod assemblies that had
evidence of tip cracking were appropriate.
E2
Engineering Support of Facilities and Equipment
E2.1 Review of Tentative Repair Activities for the Manway Cover on the Unit 2
Pressurizer
a. Insoection Scone (62001)
!
!
l                           The Catawba Unit 2 pressurizer manway cover experienced a leak during
l
i                           the end of cycle 8 shutdown for refueling. To repair the leak, the
The Catawba Unit 2 pressurizer manway cover experienced a leak during
;                           licensee elected to use an alternate method of repair consisting of a
i
the end of cycle 8 shutdown for refueling.
To repair the leak, the
;
licensee elected to use an alternate method of repair consisting of a
1
1
;                                                                                                                                 Enclosure 2
;
Enclosure 2
:
:
i
i
i
i
,
,
        ,_                                                     , w         g. . - - -             -
,_
,
w
g.
. - - -
-
,


                                              -.                               .-   . -
-.
.-
.
-
l
l
      '
'
    .
.
              .
.
,                                             22
,
22
l
l
            welded diaphragm, in lieu of a flexitallic gasket.   The licensee also
welded diaphragm, in lieu of a flexitallic gasket.
            planned to replace the bolts and nuts on the manway cover with studs and
The licensee also
            nuts.   Another issue addressed in this modification was the inspection
planned to replace the bolts and nuts on the manway cover with studs and
;            and clean-up of the boric acid which had leaked from the flange of the
nuts.
Another issue addressed in this modification was the inspection
and clean-up of the boric acid which had leaked from the flange of the
;
manway behind the insulation on the pressurizer.
The inspector
!
!
            manway behind the insulation on the pressurizer. The inspector
reviewed this modification to ensure that documentation required for
;            reviewed this modification to ensure that documentation required for
;
this repair was available, and that inspection and cleanup of the boric
!
!
            this repair was available, and that inspection and cleanup of the boric      ,
,
l           acid crystals behind the pressurizer was properly addressed.                 1
l
        b. Observations and Findinas
acid crystals behind the pressurizer was properly addressed.
1
b. Observations and Findinas
In 1987, the licensee experienced several stuck bolts on the Unit 1
'
'
            In 1987, the licensee experienced several stuck bolts on the Unit 1
pressurizer manway. At that time the licensee used the alternate method
            pressurizer manway. At that time the licensee used the alternate method
of repair delineated in the Westinghouse Technical Manual for the
            of repair delineated in the Westinghouse Technical Manual for the
pressurizer.
            pressurizer. This repair consisted of using a welded diaphragm, in lieu
This repair consisted of using a welded diaphragm, in lieu
            of a flexitallic gasket.     In addition, the licensee substituted studs
of a flexitallic gasket.
            for the bolts used in the manway flange. At that time the licensee also
In addition, the licensee substituted studs
l           realized that this same modification may some day be required for Unit
for the bolts used in the manway flange. At that time the licensee also
            2. so 10 CFR 50.59 evaluations for the alternate modification method and
l
            calculations for the stress analysis of the studs and nuts were               !
realized that this same modification may some day be required for Unit
            conducted for each Unit in 1987. The inspector reviewed this                 I
2. so 10 CFR 50.59 evaluations for the alternate modification method and
            documentation as well as the Westinghouse Pressurizer Technical Manual
calculations for the stress analysis of the studs and nuts were
  .          and drawings for this alternate method of repair. The information
conducted for each Unit in 1987.
            reviewed was found to be satisfactory.
The inspector reviewed this
                                                                                          ,
documentation as well as the Westinghouse Pressurizer Technical Manual
            The inspector was initially concerned with the licensee's tentative             I
and drawings for this alternate method of repair. The information
            plans to remove insulation only from the top and bottom of the
,
            pressurizer in order to flush the boric acid crystals from behind the
.
            insulation, and to use technical justification based on boric acid
reviewed was found to be satisfactory.
            corrosion rates documented in an EPRI document (TR-102748S) for
The inspector was initially concerned with the licensee's tentative
            acceptance of any possible damage to the pressurizer. The inspector's
plans to remove insulation only from the top and bottom of the
            concern was based on the fact that the corrosion rates given in the EPRI
pressurizer in order to flush the boric acid crystals from behind the
            document differed significantly from the corrosion rates established by
insulation, and to use technical justification based on boric acid
            Westinghouse under similar conditions and documented in NRC Generic
corrosion rates documented in an EPRI document (TR-102748S) for
            Letter 88-05 " Boric Acid Corrosion of Carbon Steel Reactor Pressure
acceptance of any possible damage to the pressurizer.
            Boundary Components in Pressurized Water Reactor Plants".     In addition,
The inspector's
            the inspector did not believe that the plan to use technical
concern was based on the fact that the corrosion rates given in the EPRI
            justification met the intent of Catawba's Nuclear Site Directive 3.3.16.
document differed significantly from the corrosion rates established by
            which stated. "When there is evidence that boric acid has run under           !
Westinghouse under similar conditions and documented in NRC Generic
            insulation remove enough insulation during the inspection 3rocess to         l
Letter 88-05 " Boric Acid Corrosion of Carbon Steel Reactor Pressure
            assure all boric acid has been identified and evaluated. S1ould the
Boundary Components in Pressurized Water Reactor Plants".
            investigation reveal no damage to the contaminated components, the area       l
In addition,
            is to be cleaned until free of visible borori crystals." During
the inspector did not believe that the plan to use technical
            discussions held with senior licensee management, the inspector was
justification met the intent of Catawba's Nuclear Site Directive 3.3.16.
            informed that the plans for boric acid damage examination and flushing
which stated. "When there is evidence that boric acid has run under
,          on the pressurizer which were identified to the inspector were very
l
          ' tentative and only one of many options being considered. The inspector         '
insulation remove enough insulation during the inspection 3rocess to
l           was also informed that a meeting on this issue was planned for following
assure all boric acid has been identified and evaluated. S1ould the
investigation reveal no damage to the contaminated components, the area
is to be cleaned until free of visible borori crystals." During
discussions held with senior licensee management, the inspector was
informed that the plans for boric acid damage examination and flushing
on the pressurizer which were identified to the inspector were very
,
' tentative and only one of many options being considered. The inspector
l
was also informed that a meeting on this issue was planned for following
i
i
            week and the decisions reached in this meeting would be forwarded to the       )
week and the decisions reached in this meeting would be forwarded to the
i          inspector for review.                                                         l
)
                                                                    Enclosure 2
inspector for review.
                                                                                          I:
i
Enclosure 2


                                                          .   .   - -           -       -
.
                                                                                          -
.
      ,
- -
    ,
-
                .
-
                                                23
-
              On April 9.1997, the inspector was informed of the licensee plans for
,
                inspection and cleaning of boric acid on the pressurizer. These plans
,
              would remove three additional sections of insulation and would allow
.
              visual inspection to be performed in spot locations from the top to the
23
              bottom of the pressurizer. The only disadvantage was visual inspection
On April 9.1997, the inspector was informed of the licensee plans for
              could only be performed on the lower side of each of the sup) ort rings
inspection and cleaning of boric acid on the pressurizer.
              except the top support ring. The licensee proposed that teclnical
These plans
l             justification be used for the acceptance of the up)er portion of each
would remove three additional sections of insulation and would allow
              support ring using the EPRI criteria which Westinglouse agreed was
visual inspection to be performed in spot locations from the top to the
bottom of the pressurizer. The only disadvantage was visual inspection
could only be performed on the lower side of each of the sup) ort rings
except the top support ring. The licensee proposed that teclnical
l
justification be used for the acceptance of the up)er portion of each
support ring using the EPRI criteria which Westinglouse agreed was
a)propriate for this corrosion wear application.
These actions resolved
,
,
              a)propriate for this corrosion wear application.    These actions resolved
!
!
              t1e inspector's concerns.
t1e inspector's concerns.
l             The licensee )lanned to flush the pressurizer shell with hot water for
l
l              four to five lours in an attempt to dissolve the crystals and remove
The licensee )lanned to flush the pressurizer shell with hot water for
              them from the carbon steel surface. To verify that the flushing process
              was effective in removing the boron, the licensee planned to collect
              water samples hourly at the base of the pressurizer and obtain data on
:              boron concentrations, expecting the concentrations to decrease over
l            time. The inspector questioned the confidence level of the validation
l
l
              plan as a function of sampling frequency, and asked if an hourly sample
four to five lours in an attempt to dissolve the crystals and remove
              would provide sufficient data to verify that boron concentrations were
them from the carbon steel surface. To verify that the flushing process
  .
was effective in removing the boron, the licensee planned to collect
              indeed decreasing over time. The licensee agreed that more frequent
water samples hourly at the base of the pressurizer and obtain data on
              sampling would yield a more robust conclusion and planned to sample the
:
i              flushing water every half hour. The ins)ector reviewed the results of
boron concentrations, expecting the concentrations to decrease over
l
l
              the pressurizer flushing, documented in )IP 2-C97-0952. and concluded
time. The inspector questioned the confidence level of the validation
              that the flushing plan was effective in removing any dried boric acid
l
!
plan as a function of sampling frequency, and asked if an hourly sample
              from the pressurizer shell.
would provide sufficient data to verify that boron concentrations were
          c. Conclusions
indeed decreasing over time. The licensee agreed that more frequent
              The inspector concluded that documentation for the modification of the
.
              Unit 2 pressurizer manway was satisfactory and engineering
sampling would yield a more robust conclusion and planned to sample the
              considerations for modification, inspection, and cleaning of the
flushing water every half hour. The ins)ector reviewed the results of
              pressurizer shell were very good. Results of the boric acid cleanup
i
              indicated that the plan had been effective.
l
        E2.2 Desian Control
the pressurizer flushing, documented in )IP 2-C97-0952. and concluded
          a. Ir;soection
that the flushing plan was effective in removing any dried boric acid
                r        Scope (37550)
!
              The inspector reviewed modifications being implemented during the Unit 2
from the pressurizer shell.
              outage. A)plicable regulatory requirements included Regulatory Guide
c. Conclusions
              1.64 and AiSI N45.2.11-1974. Quality Assurance Requirements for the
The inspector concluded that documentation for the modification of the
              Design of Nuclear Power Plants 10 CFR 50.59,10 CFR 50 Appendix B the
Unit 2 pressurizer manway was satisfactory and engineering
.             licensee's Quality Assurance Topica'l Report (Duke-1-A), and associated
considerations for modification, inspection, and cleaning of the
pressurizer shell were very good.
Results of the boric acid cleanup
indicated that the plan had been effective.
E2.2 Desian Control
a. Ir;soection Scope (37550)
r
The inspector reviewed modifications being implemented during the Unit 2
outage.
A)plicable regulatory requirements included Regulatory Guide
1.64 and AiSI N45.2.11-1974. Quality Assurance Requirements for the
Design of Nuclear Power Plants 10 CFR 50.59,10 CFR 50 Appendix B the
.
licensee's Quality Assurance Topica'l Report (Duke-1-A), and associated
l
l
I
I
i
i
;
;
                                                                      Enclosure 2
Enclosure 2


    '
'
  .
.
              .
.
                                              24
24
                                                                                      :
design control implementing procedures.
            design control implementing procedures.   The following modifications
The following modifications
            were reviewed:
were reviewed:
            .      VN 8303H   Replacement of Limitorque Motors on 2NI-54A. 2NI-65B. 1
VN 8303H
                                2NI-76A. and 2NI-183B
Replacement of Limitorque Motors on 2NI-54A. 2NI-65B.
            .      CN 21377   Modify Safety Injection (SI) Logic to Delete Low Stear )
.
                                Pressure Input                                         1
2NI-76A. and 2NI-183B
            .      CN 21375   Upgrade Allowable Temperature for Some Auxiliary Feed
CN 21377
                                Water (CA) Piping.
Modify Safety Injection (SI) Logic to Delete Low Stear
                                                                                      l
.
        b. Observations and Findinas                                                 )
Pressure Input
                                                                                      1
CN 21375
            The specified post modification testing requirements on the above         I
Upgrade Allowable Temperature for Some Auxiliary Feed
            modifications adequately verified the design function of the modified     l
.
            equipment. Implementation of the SI signal deletion (CN 21377) resulted   I
Water (CA) Piping.
            in damage to six process cards in the Solid State Protection System       l
b. Observations and Findinas
            cabinet due to short circuits experienced during wiring terminations.     l
The specified post modification testing requirements on the above
            The damaged cards were identified during post modification testing.
modifications adequately verified the design function of the modified
            Appropriate actions were initiated to replace the damaged cards and       ,
equipment.
            verify the integrity of the remaining installed cards.                   '
Implementation of the SI signal deletion (CN 21377) resulted
            Replacement Motor Operated Valve Limitorcue motors (VN 8303H) were set   '
in damage to six process cards in the Solid State Protection System
            up using the VOTES testing procedures anc implementing the applicable GL
cabinet due to short circuits experienced during wiring terminations.
            89-10 requirements. The modification was required because tie original
The damaged cards were identified during post modification testing.
            size motors for the NI valves were not available. Cracks were found on
Appropriate actions were initiated to replace the damaged cards and
            the motor shafts' key way of the installed motors. Post modification
,
            verification was accomplished by Quality Control inspections for the CA
verify the integrity of the remaining installed cards.
            piping support modifications to upgrade the allowable piping temperature
'
            (CN 21375).
Replacement Motor Operated Valve Limitorcue motors (VN 8303H) were set
            The 50.59 evaluations for the modifications were adequate. A regulatory
'
            issue was pending on the 50.59 evaluation for the CA piping upgrade (NRC
up using the VOTES testing procedures anc implementing the applicable GL
            Inspection Report 50-413.414/96-03). The SI logic signal deletion
89-10 requirements.
            safety evaluation was documented in licensing amendments 158 and 150.
The modification was required because tie original
        c. Conclusion
size motors for the NI valves were not available.
            Regulatory design control requirements were appropriately implemented
Cracks were found on
            for the Unit 2 outage modifications reviewed during this inspection.
the motor shafts' key way of the installed motors.
      E4     Engineering Staff Knowledge and Performance
Post modification
      E4.1 Identification and Correction of Eauioment Problems
verification was accomplished by Quality Control inspections for the CA
;       a. Insoection Stone (37550)
piping support modifications to upgrade the allowable piping temperature
            The inspector reviewed the licensee's actions related to the
(CN 21375).
            identification and resolution of MOV limitorque motor shaft cracking.
The 50.59 evaluations for the modifications were adequate. A regulatory
                                                                      Enclosure 2
issue was pending on the 50.59 evaluation for the CA piping upgrade (NRC
Inspection Report 50-413.414/96-03).
The SI logic signal deletion
safety evaluation was documented in licensing amendments 158 and 150.
c. Conclusion
Regulatory design control requirements were appropriately implemented
for the Unit 2 outage modifications reviewed during this inspection.
E4
Engineering Staff Knowledge and Performance
E4.1 Identification and Correction of Eauioment Problems
;
a. Insoection Stone (37550)
The inspector reviewed the licensee's actions related to the
identification and resolution of MOV limitorque motor shaft cracking.
Enclosure 2
l
l
l
l
Line 1,682: Line 2,374:


i
i
      '
'
    .
.
                .                             r
.
r
1
1
                                                  25
25
              Applicable regulatory requirements included 10 CFR 50 Appendix B and the
Applicable regulatory requirements included 10 CFR 50 Appendix B and the
              licensee's Topical Quality Assurance Program.
licensee's Topical Quality Assurance Program.
          b. Observations and Findinas
b. Observations and Findinas
industry experience reports in 1995 and late 1996 noted examples of
<
<
              industry experience reports in 1995 and late 1996 noted examples of
motor shaft key way cracking in large high speed limitorque MOV motors.
<
<
              motor shaft key way cracking in large high speed limitorque MOV motors.
The reports generally indicated the problem occurred in 3600 rpm motors
              The reports generally indicated the problem occurred in 3600 rpm motors
sized at 80 ft-lbs and larger. There were ten applications identified
              sized at 80 ft-lbs and larger. There were ten applications identified   ,
,
              at Catawba which included the four cold leg accumulator isolation valves )
at Catawba which included the four cold leg accumulator isolation valves
              and the NI-183 valves on each unit. The licensee implemented a motor
)
              shaft inspection into the GL 89-10 program in 1996. No cracks were       1
and the NI-183 valves on each unit. The licensee implemented a motor
              identified on the Unit 1 valves inspected during the previous outage.   '
shaft inspection into the GL 89-10 program in 1996.
              There were cracks identified on three Unit 2 valves inspected during the
No cracks were
              current outage. Replacement motors of the original sizes were
identified on the Unit 1 valves inspected during the previous outage.
              unavailable therefore a minor modification was implemented to change
'
              the motor sizes. The original 175 ft-lb motor on 2NI-183B was replaced
There were cracks identified on three Unit 2 valves inspected during the
              with a 150 ft-lb motor from Cold Leg Accumulator valve 2NI-54. The
current outage.
              original 150 ft-lb motors on 2NI-54A. 2NI-65B and 2NI-76A were replaced
Replacement motors of the original sizes were
              with 80 ft-lb. 80 ft-lb. and 100 ft-lb motors, respectively.     Valve
unavailable therefore a minor modification was implemented to change
              motor torque switch settings and parameters were revised to meet the
the motor sizes.
              recuirements of the GL 89-10 program and motor / valve application.
The original 175 ft-lb motor on 2NI-183B was replaced
  .          Adcitionally, the associated motor control center overload heaters were
with a 150 ft-lb motor from Cold Leg Accumulator valve 2NI-54.
              replaced on each valve to be consistent with the motor protection
The
              requirements.
original 150 ft-lb motors on 2NI-54A. 2NI-65B and 2NI-76A were replaced
          c. Conclusion                                                               4
with 80 ft-lb. 80 ft-lb. and 100 ft-lb motors, respectively.
              The identification and correction of MOV shaft key way cracking in Unit
Valve
              2 safety injection system valves was a good example of engineering
motor torque switch settings and parameters were revised to meet the
              identification and resolution of equipment problems. Industry operating
recuirements of the GL 89-10 program and motor / valve application.
              experience was appropriately incorporated into licensee activities and
Adcitionally, the associated motor control center overload heaters were
              effectively eliminated a potential safety-related equipment failure       '
.
              mechanism.
replaced on each valve to be consistent with the motor protection
        E8   Hiscellaneous Engineering Issues (92903)
requirements.
        E8.1 .(flosed) VIO 50-413.414/96-13-04: Inadequate Design Controls - Two
c. Conclusion
              Examples
4
              Example 1-Selection of Main Steam Isolation Valve (MSIV) Solenoid
The identification and correction of MOV shaft key way cracking in Unit
              Valves:   This item identified a discrepancy where the nameplate design
2 safety injection system valves was a good example of engineering
              rating of MSIV solenoid valves was less than the maximum design pressure
identification and resolution of equipment problems.
              of the instrument air system. The ins)ector reviewed the licensee's
Industry operating
              response dated November 6. 1996. The Jnit 1 solenoid valves were
experience was appropriately incorporated into licensee activities and
              replaced with aapropriate valves prior to identification of the
effectively eliminated a potential safety-related equipment failure
              discrepancy. T1e valve manufacturer certified by letter that the
'
mechanism.
E8
Hiscellaneous Engineering Issues (92903)
E8.1 .(flosed) VIO 50-413.414/96-13-04: Inadequate Design Controls - Two
Examples
Example 1-Selection of Main Steam Isolation Valve (MSIV) Solenoid
Valves:
This item identified a discrepancy where the nameplate design
rating of MSIV solenoid valves was less than the maximum design pressure
of the instrument air system. The ins)ector reviewed the licensee's
response dated November 6. 1996.
The Jnit 1 solenoid valves were
replaced with aapropriate valves prior to identification of the
discrepancy.
T1e valve manufacturer certified by letter that the
l
l
              existing Unit 2 solenoid valves were acceptable until replacement at the
existing Unit 2 solenoid valves were acceptable until replacement at the
i
i
              next refueling outage. The inspector verified that the Unit 2 solenoid
next refueling outage. The inspector verified that the Unit 2 solenoid
l             valves were replaced with upgraded valves during this refueling outage
l
                                                                      Enclosure 2
valves were replaced with upgraded valves during this refueling outage
l
l
Enclosure 2


i
i
      '
'
l   .
l
                .
.
l                                                 26
.
                                                                                        '
l
              (MW0s 96070278. 96070289. 96070280. 96070287) and testing of the
26
              replacement solenoid valves was performed satisfactorily (PT
'
              2/A/4200/09. Engineered Safety Feature Actuation Periodic Test).
(MW0s 96070278. 96070289. 96070280. 96070287) and testing of the
              Examole 2-Standby Shutdown System (SSS) Make-uo Pumn . Calculation - This
replacement solenoid valves was performed satisfactorily (PT
              item identified calculation design input errors '       'd to the system
2/A/4200/09. Engineered Safety Feature Actuation Periodic Test).
              conditions and pulsation damper which were useo   4
Examole 2-Standby Shutdown System (SSS) Make-uo Pumn . Calculation - This
                                                                    .wify the Net
item identified calculation design input errors '
              Positive Suction Head (NPSH) for the SSS make-up pum). The licensee's
'd to the system
              November 6. 1996, response to the violation stated tie design inputs for
conditions and pulsation damper which were useo
              the SSS make-up pum) sizing calculation and the damper design would be
.wify the Net
              evaluated and opera]ility for the Unit 1 and 2 pumps verified. The
4
              inspector reviewed the licensee's completed corrective actions and
Positive Suction Head (NPSH) for the SSS make-up pum). The licensee's
              verified that the in)ut errors were resolved. Additionally, the actions
November 6. 1996, response to the violation stated tie design inputs for
              to assure pump opera]ility were completed.
the SSS make-up pum) sizing calculation and the damper design would be
        E8.2 (Closed) DEV 50-413.414/92-01-03.: Breaker Coordination
evaluated and opera]ility for the Unit 1 and 2 pumps verified. The
              This deviation was closed based on NRC Inspection Report 50-413.414/96-
inspector reviewed the licensee's completed corrective actions and
              19.
verified that the in)ut errors were resolved. Additionally, the actions
        E8.3 (Closed) VIO 50-413.414/96-12-03: Inadequate Design Controls For
to assure pump opera]ility were completed.
              Ensuring Containment Crane Wall And Floor Drain Screens Implemented
E8.2 (Closed) DEV 50-413.414/92-01-03.: Breaker Coordination
  .            Design Requirements.                                                       l
This deviation was closed based on NRC Inspection Report 50-413.414/96-
              This item identified containment crane wall penetrations and floor drain i
19.
              screens that did not implement design requirements developed to preclude   ;
E8.3 (Closed) VIO 50-413.414/96-12-03: Inadequate Design Controls For
              transport of debris to the Emergency Core Cooling System sum) screens.     l
Ensuring Containment Crane Wall And Floor Drain Screens Implemented
              The licensee's October 29, 1996. violation response stated tlat the       !
Design Requirements.
              crane wall Jenetrations were filled with cualified foam to preclude any
.
              flow throug1 them and modifications were ceveloped correct the screen
This item identified containment crane wall penetrations and floor drain
              size of the floor drain screens. The inspector reviewed the licensee's     j
i
              completed corrective actions, including minor modifications (CNCE-8116.   )
screens that did not implement design requirements developed to preclude
              8139. 8186) and drawing revisions (CN-1070-5. rev. 14). The inspector
transport of debris to the Emergency Core Cooling System sum) screens.
              also performed a walkdown of the unit 2 containment building and
The licensee's October 29, 1996. violation response stated tlat the
              verified that the modifications were installed.
crane wall Jenetrations were filled with cualified foam to preclude any
                                          IV. Plant Support
flow throug1 them and modifications were ceveloped correct the screen
        R1     Radiological Protection and Chemistry Controls
size of the floor drain screens.
        R1.1 Tour of Ridioloaical Protected Areas
The inspector reviewed the licensee's
          a. Insoection Scooe (83750. 71750)
j
              The inspectors reviewed implementation of selected elements of the
completed corrective actions, including minor modifications (CNCE-8116.
              licensee's radiation protection program as required by 10 Code of
)
              Federal Regulations (CFR) Parts 20.1201. 1208, 1501. 1502. 1601, 1703.
8139. 8186) and drawing revisions (CN-1070-5. rev. 14).
i             1802. 1902, and 1904. The review included observation of radiological
The inspector
              protection activities, including personnel monitoring controls, control
also performed a walkdown of the unit 2 containment building and
verified that the modifications were installed.
IV. Plant Support
R1
Radiological Protection and Chemistry Controls
R1.1 Tour of Ridioloaical Protected Areas
a. Insoection Scooe (83750. 71750)
The inspectors reviewed implementation of selected elements of the
licensee's radiation protection program as required by 10 Code of
Federal Regulations (CFR) Parts 20.1201. 1208, 1501. 1502. 1601, 1703.
i
1802. 1902, and 1904.
The review included observation of radiological
protection activities, including personnel monitoring controls, control
:
:
                                                                        Enclosure 2
Enclosure 2


    _ _ _ _ .__ _ __ _ .. _ . - _ _ _ _ . _ _ _._ _ _ _ . _ _ _ . _
_ _ _ _ .__ _ __ _ .. _ . - _ _ _ _ . _ _ _._ _ _ _ . _ _ _ . _
                                                                                                                          '
l
l
P                         ,                                                                                               ;
'
                                                                                                                          *
P
                      ,
,
                                                                                                                          >
;
                                              .
*
,
l.
l.
L                                                                                   27
.
                                            of ra'dioactive material, radiological postings, and radiation area /high
>
                                            radiation area controls,
L
                                    b. Observations and Findinas
27
                                            During tours of the Auxiliary Building and radioactive waste                 !
of ra'dioactive material, radiological postings, and radiation area /high
                                            storage /handhng facilities. the inspector reviewed survey data and           '
radiation area controls,
                                            performed selected independent radiation and contamination surveys of
b. Observations and Findinas
                                            radioactive material storage areas. Observations and survey results
During tours of the Auxiliary Building and radioactive waste
                                            determined-the licensee was effectively controlling and storing
!
                                            radioactive material.                                                         '
storage /handhng facilities. the inspector reviewed survey data and
i                                                                               -             -
'
performed selected independent radiation and contamination surveys of
radioactive material storage areas.
Observations and survey results
determined-the licensee was effectively controlling and storing
radioactive material.
'
i
-
-
i
i
                          .              ~The inspector reviewed records for selected employees who had recently         ;
~The inspector reviewed records for selected employees who had recently
.
;
!
worn respiratory protection equipment. The inspector verified that for -
<
the records reviewed, each worker had successfully completed respiratory
l
protection training, was medically qualified, and was fit-tested for the
l
specific respirator type used in accordance with licensee procedural
!
!
                                          worn respiratory protection equipment. The inspector verified that for -        <
requirements. All respiratory protection equipment observed during
                                            the records reviewed, each worker had successfully completed respiratory
facility tours was being maintained in a satisfactory condition.
l                                          protection training, was medically qualified, and was fit-tested for the
The
l                                          specific respirator type used in accordance with licensee procedural
-
!                                          requirements. All respiratory protection equipment observed during
licensee had continued to implement engineering controls for respirator
                                            facility tours was being maintained in a satisfactory condition. The         -
reductions.
                                            licensee had continued to implement engineering controls for respirator
During plant tours, the inspector observed that Extra High Radiation
                                            reductions.
.
  .                                        During plant tours, the inspector observed that Extra High Radiation
,
,
                                          Areas were locked as required by licensee procedures. The inspector
Areas were locked as required by licensee procedures. The inspector
l                                           also observed dosimetry controls for these areas were also established
l
also observed dosimetry controls for these areas were also established
in Radiation Work Permits (RWPs) as required by licensee procedures.
E
E
                                            in Radiation Work Permits (RWPs) as required by licensee procedures.          t
t
                                          The licensee's records indicated that the licensee was maintaining             :
The licensee's records indicated that the licensee was maintaining
                                            approximately 145,000 square feet (ft2 ) of floor space as a
:
P                                         Radiologically Controlled Area (RCA). Records also showed that the
2
                                            licensee maintained approximately 800-1000 ft2 (or less than 1 percent)
approximately 145,000 square feet (ft ) of floor space as a
                                            of the RCA as contaminated area during non-outage periods. During the-
P
                                            current       outage period, the licensee was maintaining approximately 1200
Radiologically Controlled Area (RCA).
Records also showed that the
licensee maintained approximately 800-1000 ft2 (or less than 1 percent)
of the RCA as contaminated area during non-outage periods.
During the-
current outage period, the licensee was maintaining approximately 1200
'
'
                                                2
2
.                                           ft as     contaminated area.
.
t                                          The inspectors reviewed Personnel Contamination Event (PCE) reports
ft as contaminated area.
                                          prepared by the licensee to track, trend, determine root cause, and any
The inspectors reviewed Personnel Contamination Event (PCE) reports
                                          necessary followup action. Approximately 49 PCEs had occurred in 1997:
t
                                            of which, approximately 38 PCEs had occurred during the current Unit 2
prepared by the licensee to track, trend, determine root cause, and any
                                          outage. The inspectors reviewed PCE log sheets for the past three years
necessary followup action. Approximately 49 PCEs had occurred in 1997:
                                            and noted PCEs continued to trend downward. The licensee attributed
of which, approximately 38 PCEs had occurred during the current Unit 2
                                          this reduction to several planned contamination control initiatives,
outage.
The inspectors reviewed PCE log sheets for the past three years
and noted PCEs continued to trend downward. The licensee attributed
this reduction to several planned contamination control initiatives,
.uch as: increased followup with workers following contamination events:
,
,
                                            .uch as: increased followup with workers following contamination events:
reduction of contaminated areas: and reductions in radioactive waste.
!
During facility tours. the inspectors observed that survey
instrumentation and continuous air monitors observed in use within the
-
!
!
                                            reduction of contaminated areas: and reductions in radioactive waste.
RCA were operable and currently calibrated. The inspectors observed a
                                          During facility tours. the inspectors observed that survey
survey instrument (portable frisker) in the Unit 2 Reactor Containment
                                            instrumentation and continuous air monitors observed in use within the
(
                                                                    -
Building which had not been source checked as required by licensee
!                                          RCA were operable and currently calibrated. The inspectors observed a
Enclosure 2
                                            survey instrument (portable frisker) in the Unit 2 Reactor Containment
(                                         Building which had not been source checked as required by licensee
                                                                                                          Enclosure 2
t
t
I
I
                                                          _-                           .
9=
                                                      9=                                  --9
_-
.
--9


    .     _       .~ -                 -     .         - .. -.     . _ _ , .__ -         _ .-
.
                                                                                                  l
_
            '
.~ -
        ,
-
                        .
.
                                                        28
- .. -.
      -
. _ _ , .__
                      Procedure HP/0/B1003/22. Paragraph 4.9.   The licensee conducted an
-
                      immediate investigation and located another frisker in the Unit 2
_
                      Reactor Containment Building which was available for use in the area       !
.-
                      that had not been source checked. The licensee removed both instruments
'
                      from the work area and performed a source check of the instruments to
,
                      verify operability. Both instruments source checked satisfactorily.
.
                      The licensee also initiated a Problem Investigation Process (PIP) report
28
                      to investigate the problem. The inspectors informed the licensee that     ;
Procedure HP/0/B1003/22. Paragraph 4.9.
                      using survey instruments that had not been source checked was a
The licensee conducted an
                      violation of licensee procedure and TS 6.8.1. Procedures and Programs.
-
                      However, based on the licensee's immediate corrective actions and the
immediate investigation and located another frisker in the Unit 2
                      safety significance of the circumstances. this licensee identified and
Reactor Containment Building which was available for use in the area
                      corrected violation is being treated as a Non-Cited Violation consistent   ,
that had not been source checked.
                    with Section VII.B.1 of the NRC Enforcement Policy. NCV 50-413.414/97-
The licensee removed both instruments
                      07-04: Failure to Source Check Survey Instruments as Required by
from the work area and performed a source check of the instruments to
                      Licensee Procedures.
verify operability.
                      The ins)ectors reviewed controls for entering the RCA and performing
Both instruments source checked satisfactorily.
                    work. T1ese controls included the use of RWPs to be reviewed and
The licensee also initiated a Problem Investigation Process (PIP) report
                      understood by workers prior to entering the RCA. The inspectors
to investigate the problem. The inspectors informed the licensee that
                      reviewed selected RWPs for adequacy of the radiation protection
;
                      requirements based on work scope, location, and conditions. For the
using survey instruments that had not been source checked was a
  .                  RWPs reviewed, the inspectors noted that appropriate protective
violation of licensee procedure and TS 6.8.1. Procedures and Programs.
                      clothing and dosimetry were required. During tours of the plant, the
However, based on the licensee's immediate corrective actions and the
                      inspectors observed the adherence of plant workers to the RWP
safety significance of the circumstances. this licensee identified and
                      requirements. The inspectors also verified the licensee was effectively
corrected violation is being treated as a Non-Cited Violation consistent
,.                    managing controls for any declared pregnant women in regards to
                      embryo / fetus doses as required by 10 CFR 20.1208. The licensee was
,                    holding current personnel dosimetry accreditation from the National
:                    Voluntary Laboratory Accreditation Program (NVLAP) as required by 10 CFR
                      20.1501.
                c. Conclusions
                      Based on observations and procedural reviews, the inspectors determined
                      the licensee was effectively maintaining controls for personnel
                      monitoring. respiratory protection, control of radioactive material,
                      radiological postings, and radiation area /high radiation area controls
                      as required by 10 CFR Part 20. One NCV was identified for failure to
                      source check survey instruments as required by licensee procedure.
              R1.2 Occuoational Radiation Exoosure Control Proaram
l              a. Insoection Scooe (83750)
                      The inspectors reviewed the licensee's implementation of 10 CFR
;'                    20.1101(b) which requires that the licensee shall use, to the extent
                      practicable, procedures and engineering controls based upon sound
                      radiation protection principles to achieve occupational doses and doses
,
,
                                                                                Enclosure 2
with Section VII.B.1 of the NRC Enforcement Policy.
NCV 50-413.414/97-
07-04:
Failure to Source Check Survey Instruments as Required by
Licensee Procedures.
The ins)ectors reviewed controls for entering the RCA and performing
work. T1ese controls included the use of RWPs to be reviewed and
understood by workers prior to entering the RCA.
The inspectors
reviewed selected RWPs for adequacy of the radiation protection
requirements based on work scope, location, and conditions.
For the
RWPs reviewed, the inspectors noted that appropriate protective
.
clothing and dosimetry were required.
During tours of the plant, the
inspectors observed the adherence of plant workers to the RWP
requirements.
The inspectors also verified the licensee was effectively
managing controls for any declared pregnant women in regards to
,.
embryo / fetus doses as required by 10 CFR 20.1208. The licensee was
holding current personnel dosimetry accreditation from the National
,
:
Voluntary Laboratory Accreditation Program (NVLAP) as required by 10 CFR
20.1501.
c. Conclusions
Based on observations and procedural reviews, the inspectors determined
the licensee was effectively maintaining controls for personnel
monitoring. respiratory protection, control of radioactive material,
radiological postings, and radiation area /high radiation area controls
as required by 10 CFR Part 20.
One NCV was identified for failure to
source check survey instruments as required by licensee procedure.
R1.2 Occuoational Radiation Exoosure Control Proaram
l
a. Insoection Scooe (83750)
The inspectors reviewed the licensee's implementation of 10 CFR
;'
20.1101(b) which requires that the licensee shall use, to the extent
practicable, procedures and engineering controls based upon sound
radiation protection principles to achieve occupational doses and doses
,
Enclosure 2
l
l
:
:
l
l
l
l
                                                                                                  1


                          .-       _ _   .. . _ _ _ _   _.     _.   __       _ _ ___
.-
    0
_ _
              .
.. . _ _ _ _
                                                        29
_.
            to members of the public that are As Low As Reasonably Achievable
_.
            (ALARA).
__
        b. Observations and Findinas
_
            The inspectors review of the licensee's ALARA program determined that
_
            the licensee had established an annual exposure goal of approximately
___
            286 person-rem, which included the Unit 2 outage goal of 132 person-rem
0
            and Jart of a planned Unit 1 outage to begin late in 1997. At the time
.
            of t1e inspection the licensee was tracking approximately 9 person-rem
29
            below previous estimates. The licensee had continued to track and trend
to members of the public that are As Low As Reasonably Achievable
            outage exposures for purposes of future outage preplanning and it was
(ALARA).
            determined that exposures continue to trend downward based on ALARA
b. Observations and Findinas
            initiatives. Several ALARA initiatives reviewed during the inspection
The inspectors review of the licensee's ALARA program determined that
            that attributed to lower personnel exposures included: improved
the licensee had established an annual exposure goal of approximately
            scheduling to optimize the use of shielding and reduce worker congestion
286 person-rem, which included the Unit 2 outage goal of 132 person-rem
            in areas; replacement of stellite valve components with components made
and Jart of a planned Unit 1 outage to begin late in 1997.
            from low to no stellite materials: a successful crudburst during the
At the time
            Unit 2 shutdown which reduced Unit 2 dose rates by approximately 15
of t1e inspection the licensee was tracking approximately 9 person-rem
            percent lower than previous Unit 2 outages; increased use of shielding:
below previous estimates. The licensee had continued to track and trend
            and a improved method for workers to initiate ALARA suggestions.
outage exposures for purposes of future outage preplanning and it was
  .          During tours of the facility the inspectors also observed Radiation
determined that exposures continue to trend downward based on ALARA
            protection (RP) technicians controlling access to work areas to minimize
initiatives.
            Personnel exposure and briefing workers in the work areas as
Several ALARA initiatives reviewed during the inspection
            radiological conditions changed. The inspectors also observed personnel
that attributed to lower personnel exposures included: improved
            beir.g briefed on ALARA considerations during specific briefings             l
scheduling to optimize the use of shielding and reduce worker congestion
            conducted to address RWP requirements.
in areas; replacement of stellite valve components with components made
        c. Conclusions                                                                   ,
from low to no stellite materials: a successful crudburst during the
                                                                                          l
Unit 2 shutdown which reduced Unit 2 dose rates by approximately 15
            Based on licensee planning efforts to reduce source term and the             )
percent lower than previous Unit 2 outages; increased use of shielding:
            licensee's efforts to achieve established exposure goals which were
and a improved method for workers to initiate ALARA suggestions.
            challenging, the inspectors determined the licensee was maintaining
During tours of the facility the inspectors also observed Radiation
            programs for controlling exposures ALARA and continued to be effective
.
j           in controlling overall collective dose.
protection (RP) technicians controlling access to work areas to minimize
      R5     Staff Training and Qualification in Radiation Protection                       j
Personnel exposure and briefing workers in the work areas as
        a. Insoection Scoce (83750 and 84750)
radiological conditions changed.
                                                                                            ,
The inspectors also observed personnel
            Training was reviewed to determine whether radiation protection
beir.g briefed on ALARA considerations during specific briefings
            technicians had been instructed in radiation procedures to minimize           ,
conducted to address RWP requirements.
            radiation exposures and control radioactive material as required by 10       '
c. Conclusions
            CFR 19.12.
,
Based on licensee planning efforts to reduce source term and the
licensee's efforts to achieve established exposure goals which were
challenging, the inspectors determined the licensee was maintaining
programs for controlling exposures ALARA and continued to be effective
j
in controlling overall collective dose.
R5
Staff Training and Qualification in Radiation Protection
j
a. Insoection Scoce (83750 and 84750)
,
Training was reviewed to determine whether radiation protection
technicians had been instructed in radiation procedures to minimize
,
radiation exposures and control radioactive material as required by 10
'
CFR 19.12.
t
t
'
'
        b. Observations and Findinas
b. Observations and Findinas
            The inspectors reviewed training requirements for RP technicians and the     4
The inspectors reviewed training requirements for RP technicians and the
            continuing training curriculum for the period of January 1,1996.
4
                                                                      Enclosure 2
continuing training curriculum for the period of January 1,1996.
Enclosure 2
!
!
l
l
l
l


              -
-
                                                                                      _ __
_
      '
__
    .
'
                .
.
                                                  30
.
                through April 5, 1997, which included industry events and topics to
30
                minimize radiation exposure. The inspectors also interviewed RP
through April 5, 1997, which included industry events and topics to
                personnel and observed work practices to determine the effectiveness of
minimize radiation exposure.
                continuing training.                                                       i
The inspectors also interviewed RP
          c. Conclusions
personnel and observed work practices to determine the effectiveness of
                Based on the training activities reviewed, the inspectors determined
continuing training.
                radiation protection technicians were receiving an appropriate level of     l
i
                training to perform routine work activities involving radiation and/or
c. Conclusions
                radioactive material.
Based on the training activities reviewed, the inspectors determined
        R7     Quality Assurance in Radiation Protection and Chemistry
radiation protection technicians were receiving an appropriate level of
          a. Insoection Scooe (83750)
training to perform routine work activities involving radiation and/or
                                                                                            :
radioactive material.
                10 CFR 20.1101 requires that the licensee periodically review the RP
R7
                program content and implementation at least annually. Licensee periodic
Quality Assurance in Radiation Protection and Chemistry
                reviews of the RP program were reviewed to determine the edequacy of         l
a. Insoection Scooe (83750)
                identification and corrective actions.                                       '
10 CFR 20.1101 requires that the licensee periodically review the RP
          b. Observations and Findinas
program content and implementation at least annually.
  .
Licensee periodic
                By reviewing RP procedures, observing work, reviewing industry
reviews of the RP program were reviewed to determine the edequacy of
                documentation, and performing plant walkdowns to include surveillance of
identification and corrective actions.
                work areas by supervisors and technicians during normal work coverage,       i
'
                the inspector determined that Quality Assurance audits and Self-             l
b. Observations and Findinas
                Assessment efforts in the area of RP were accomplished. Documentation
.
                of problems by licensee representatives was included in Quality
By reviewing RP procedures, observing work, reviewing industry
                Assurance Audits and Self-Assessment Reports. Corrective actions were
documentation, and performing plant walkdowns to include surveillance of
                included in the licensee's Problem Investigative Process and were being
work areas by supervisors and technicians during normal work coverage,
                completed in a timely manner.
the inspector determined that Quality Assurance audits and Self-
                During the inspection, the inspector reviewed the licensee's self-
Assessment efforts in the area of RP were accomplished.
                assessment processes for evaluating an event in which unsuspected resin
Documentation
                was found in the 2B containment spray heat exchanger on April 10, 1997.
of problems by licensee representatives was included in Quality
                The resin was analyzed by gamma isotopic analysis and determined to be
Assurance Audits and Self-Assessment Reports.
                mixed bed resin. The licensee began immediate followup actions to
Corrective actions were
                determine the extent of a Jotential spread of resins into plant systems
included in the licensee's Problem Investigative Process and were being
                that could be affected. T1e licensee formed a Failure Investigation
completed in a timely manner.
                Process Team to determine the source of the resin and to develop a
During the inspection, the inspector reviewed the licensee's self-
                recovery plan. The team was divided into key areas to identify the root
assessment processes for evaluating an event in which unsuspected resin
                cause, evaluate sluicing operations and alignments that could affect the
was found in the 2B containment spray heat exchanger on April 10, 1997.
                potential spread of resin, identify potentially degraded ecuipment.
The resin was analyzed by gamma isotopic analysis and determined to be
                identify components that could be potentially impacted, anc develop a
mixed bed resin.
The licensee began immediate followup actions to
determine the extent of a Jotential spread of resins into plant systems
that could be affected.
T1e licensee formed a Failure Investigation
Process Team to determine the source of the resin and to develop a
recovery plan.
The team was divided into key areas to identify the root
cause, evaluate sluicing operations and alignments that could affect the
potential spread of resin, identify potentially degraded ecuipment.
identify components that could be potentially impacted, anc develop a
cleanup plan.
The licensee's investigation revealed that the probable
,
,
'
'
                cleanup plan. The licensee's investigation revealed that the probable
source of the resin was a potential tear in a screenwire used to contain
                source of the resin was a potential tear in a screenwire used to contain
!
!               mixed resin inside of an ion exchanger. The ion exchanger is used
mixed resin inside of an ion exchanger. The ion exchanger is used
'
during spent fuel pool cleanup evolutions. The licensee determined that
i
i
'
only a small amount of resin was present in the containment spray
                during spent fuel pool cleanup evolutions. The licensee determined that
Enclosure 2
                only a small amount of resin was present in the containment spray
                                                                        Enclosure 2
1
1
                                                          .
.


                                                                                          !
!
(     i                                                                                   l
l
-.                                                                                     :
(
                                                                                          '
i
l
-.
:
L
L
                                                                                          i
'
                                                31
i
                                                                                          l
31
l              system, and cleanup actions were initiated to remove the resin that had   l
l
system, and cleanup actions were initiated to remove the resin that had
l
1
1
been identified. A total of approximately 200 - 250 milliliters of
o
o
                been identified. A total of approximately 200 - 250 milliliters of
resin was removed from the spent fuel pool purification and containment
                resin was removed from the spent fuel pool purification and containment   !
!
spray systems.
The licensee initiated actions to clean out ion
6
<
<
                spray systems.  The licensee initiated actions to clean out ion          6
l              exchanger post filter housings whenever filters are changed to help        i
l              eliminate the potential for the small amounts of resin from entering      l
l
l
exchanger post filter housings whenever filters are changed to help
i
l
eliminate the potential for the small amounts of resin from entering
l
l
into the containment s] ray system. The licensee's engineering
;
'
'
                into the containment s] ray system. The licensee's engineering            ;
evaluation concluded tlat there were no operability concerns resulting
              evaluation concluded tlat there were no operability concerns resulting     .
.
i              from this event, and the inspector concluded that the licensee's review
from this event, and the inspector concluded that the licensee's review
l               for operability was logical. The inspector determined that the licensee   !
i
l
for operability was logical.
The inspector determined that the licensee
!
was aggressive in performing a root cause analysis of the resin event.
!
!
!
              was aggressive in performing a root cause analysis of the resin event.    !
l
l              and the licensee's assessments of the event were good.                     i
and the licensee's assessments of the event were good.
                                                                                          !
i
            c. Conclusions                                                               i
!
                                                                                          !
c. Conclusions
              The inspector determined the licensee was performing Quality Assurance     !
i
              Audits and effectively assessing the radiation protection program as       !
!
              required by 10 CFR Part 20.1101. The inspector also determined the         :
The inspector determined the licensee was performing Quality Assurance
                licensee was completing corrective actions in a timely manner.
!
                                                                                          l
Audits and effectively assessing the radiation protection program as
        F2   Status of Fire Protection Facilities and Equipment
required by 10 CFR Part 20.1101. The inspector also determined the
:
licensee was completing corrective actions in a timely manner.
l
F2
Status of Fire Protection Facilities and Equipment
'
f
'.
'.
  '
F2.1 00erability of Fire Protection Facilities and Ecuioment
        F2.1 00erability of Fire Protection Facilities and Ecuioment
a. Inspection Scoce (64704)
                                                                                          f
i
            a. Inspection Scoce (64704)                                                   i
i
                                                                                          i
The inspectors reviewed open corrective maintenance work orders on fire
                                                                                          '
'
              The inspectors reviewed open corrective maintenance work orders on fire
protection components and operation's list of out-of-service fire
              protection components and operation's list of out-of-service fire
protection equipment to assess the licensee's performance for returning
              protection equipment to assess the licensee's performance for returning
degraded fire protection components to service.
              degraded fire protection components to service. In addition, walkdown     !
In addition, walkdown
              inspections were made to assess the material condition of the plant's     l
!
              fire protection systems, equipment, features and fire brigade equipment.   t
inspections were made to assess the material condition of the plant's
        b.   Observations and Findinos                                                 !
l
              Maintenance and Ooerability of Fire Protection Ecuioment and Comoonents
fire protection systems, equipment, features and fire brigade equipment.
                                                                                          l
t
              As of March 31, 1997, there were approximately 22 fire protection          )
b.
              related work requests-in which the work had not been completed. Most of  ' i'
Observations and Findinos
              these involved minor corrective maintenance work items and did not
!
!
              affect the operability of the components. All of these work requests.       i
Maintenance and Ooerability of Fire Protection Ecuioment and Comoonents
              except for work request item 910001140, were initiated in 1997 or late
l
:              1996. Item 910001140 involved repairs to the fire pump suction screens
As of March 31, 1997, there were approximately 22 fire protection
)
related work requests-in which the work had not been completed. Most of
these involved minor corrective maintenance work items and did not
' i'
!
!
              which were to be corrected by minor modification CE-3197. This work had
affect the operability of the components.
              been completed except for the proper reinstallation of the suction
All of these work requests.
              screens. As of the date of this inspection, these screens had not been      ,
i
i             fully installed to the botsom of the screen frame. This resulted in an      !
except for work request item 910001140, were initiated in 1997 or late
              estimated area approximately 78x11 feet in size near the bottom of the
              pump suction pit not being filtered.
                                                                                          i
:
:
                                                                                          l
1996.
                                                                        Enclosure 2
Item 910001140 involved repairs to the fire pump suction screens
                                                                                          !
which were to be corrected by minor modification CE-3197. This work had
                                                                                          !
!
                                                                                          '
been completed except for the proper reinstallation of the suction
screens.
As of the date of this inspection, these screens had not been
,
,
                                                        .
i
fully installed to the botsom of the screen frame.
This resulted in an
!
estimated area approximately 78x11 feet in size near the bottom of the
pump suction pit not being filtered.
i
:
Enclosure 2
l
!
!
'
,
.


                                                        ._ -         -   .-   - .
._
      .                                               l
-
    .
-
          .
.-
                                          32
-
        Two of the three fire pumps take suction from the fire protection
.
        suction pit. This suction pit was provided with two suction screens
l
        with 3/8-inch mesh installed to filter and prevent raw lake water trash
.
        and debris from entering the suction pit for the pumps and clogging the
.
        suction inlets for the two pumps. The third fire pump takes suction
.
        from the suction pit for the low pressure service water pumps.
32
        The fire pump suction screens were found degraded in late 1990 and
Two of the three fire pumps take suction from the fire protection
        repairs were initiated in 1991. Following these repairs. the suction         '
suction pit.
        screens were not properly reinstalled. Reportedly, a lifting beam
This suction pit was provided with two suction screens
        device was misplaced during the modification process.   Without the beam
with 3/8-inch mesh installed to filter and prevent raw lake water trash
        device the filters could not be properly installed.   The Catawba Fire
and debris from entering the suction pit for the pumps and clogging the
        Protection OA Program has been incorporated into the Duke Topical Report
suction inlets for the two pumps.
        GA Program as OA Condition 3.     The Topical Report. Section 17.3.1.6
The third fire pump takes suction
        states that Duke has established a corrective action process whereby all     i
from the suction pit for the low pressure service water pumps.
        personnel are to assure conditions adverse to quality are promptly
The fire pump suction screens were found degraded in late 1990 and
        identified, controlled, and corrected. Also. Topical Report Section
repairs were initiated in 1991.
        17.3.2.13 - Corrective Action. requires conditions adverse to quality to
Following these repairs. the suction
        be corrected The failure to correct the degraded filter screens for
'
        the fire pumps in a timely manner is identified as Violation 50-
screens were not properly reinstalled.
        413.414/97-07-05. Following this inspection, the licensee notified the
Reportedly, a lifting beam
        inspectors that these screens were properly installed on May 14. 1997.
device was misplaced during the modification process.
  .
Without the beam
        Otherwise, the inspectors concluded that there was no significant
device the filters could not be properly installed.
        maintenance backlog associated with fire protection components.
The Catawba Fire
        Also, as of March 31. 1997, there were 22 degraded or inoperable fire
Protection OA Program has been incorporated into the Duke Topical Report
        protection components. Most of these items were related to the Unit 2
GA Program as OA Condition 3.
        refueling outage which was in progress. For example several fire
The Topical Report. Section 17.3.1.6
        barrier penetrations were open for movement of materials through open
states that Duke has established a corrective action process whereby all
        floor hatches and the CO2 system for the 2A diesel generator was removed
i
        from service due to maintenance work being performed on the diesel
personnel are to assure conditions adverse to quality are promptly
        engine. The remaining degraded features were either in nonsafety-
identified, controlled, and corrected. Also. Topical Report Section
        related areas or were minor discrepancies which did not affect the             !
17.3.2.13 - Corrective Action. requires conditions adverse to quality to
        operability of the system or component. Four of these items had been           l
be corrected
        degraded since late 1996. the remainder had been degraded since early           i
The failure to correct the degraded filter screens for
        1997   The inspectors verified that appropriate com)ensatory measures         i
the fire pumps in a timely manner is identified as Violation 50-
        had been implemented for the degraded components, w1ere required. One         I
413.414/97-07-05.
        degraded component required a continuous fire watch and three degraded         '
Following this inspection, the licensee notified the
        components required an hourly fire watch patrol. The remaining degraded       I
inspectors that these screens were properly installed on May 14. 1997.
        components were considered operable and did not require any compensatory
.
        actions.                                                                       l
Otherwise, the inspectors concluded that there was no significant
                                                                                      '
maintenance backlog associated with fire protection components.
        The inspectors toured the plant and noted that the operable fire
Also, as of March 31. 1997, there were 22 degraded or inoperable fire
;       protection systems were well maintained and the material condition was
protection components.
;       very good.
Most of these items were related to the Unit 2
refueling outage which was in progress.
For example several fire
barrier penetrations were open for movement of materials through open
floor hatches and the CO system for the 2A diesel generator was removed
2
from service due to maintenance work being performed on the diesel
engine. The remaining degraded features were either in nonsafety-
related areas or were minor discrepancies which did not affect the
operability of the system or component.
Four of these items had been
degraded since late 1996. the remainder had been degraded since early
1997
The inspectors verified that appropriate com)ensatory measures
had been implemented for the degraded components, w1ere required.
One
degraded component required a continuous fire watch and three degraded
'
components required an hourly fire watch patrol. The remaining degraded
components were considered operable and did not require any compensatory
actions.
'
The inspectors toured the plant and noted that the operable fire
;
protection systems were well maintained and the material condition was
;
very good.
l
l
                                                                Enclosure 2
Enclosure 2
l
l


                _       . .           ~     _     __ _ . _ _ _ _ , _ _ _ _ _ . _             _ _ -
_
      '
. .
    .
~
                  .
_
                                                33
__ _ . _ _ _ _ , _ _ _ _ _ . _
                                                                                                    i
_
              Fire Briaade Eauioment:                                                               !
_
              The fire brigade turnout gear was stored in a fire brigade equipment
-
              building adjacent to the Unit 2 Turbine Building. A sufficient number                 ,
'
              of turnout gear, consisting of coats, Sants boots, helmets, etc., was                 !
.
              provided to equip the fire brigade mem)ers expected to respond in the                 i
.
              event of a fire or other emergency. The equipment was properly stored                 '
33
              and well maintained.
Fire Briaade Eauioment:
        c.   Conclusions
The fire brigade turnout gear was stored in a fire brigade equipment
              The low number of open maintenance work orders and degraded fire
building adjacent to the Unit 2 Turbine Building. A sufficient number
              protection components, in conjunction with the good material condition
,
              of the fire protection components and fire brigade equipment, indicated
of turnout gear, consisting of coats, Sants boots, helmets, etc., was
              that, in general, appropriate em)hasis had been placed on the
provided to equip the fire brigade mem)ers expected to respond in the
              maintenance and operability of tie fire protection equipment and
i
              components.
event of a fire or other emergency. The equipment was properly stored
              The work to repair the suction screens for two of the three fire pump's
'
              suction piping had been o)en since 1991 and was not complete. The lack
and well maintained.
              of prompt resolution of t1e work was identified as a violation.
c.
  .
Conclusions
        F2.2 Surveillance of Fire Protection Features and Eauioment
The low number of open maintenance work orders and degraded fire
        a.   Insoection Scone (64704)
protection components, in conjunction with the good material condition
              The inspectors reviewed the following completed surveillance and test
of the fire protection components and fire brigade equipment, indicated
              procedures:
that, in general, appropriate em)hasis had been placed on the
              -
maintenance and operability of tie fire protection equipment and
                    IP/0/A/3350/13. Revision Change 0 Retype 5. EFA System Detector
components.
                    Test Procedure, Data Gathering Panel 10. Completed January 20,
The work to repair the suction screens for two of the three fire pump's
                    1997.
suction piping had been o)en since 1991 and was not complete. The lack
              -
of prompt resolution of t1e work was identified as a violation.
                    IP/0/A/3350/16. Revision Change 0 Retype 2. EFA System Detector
F2.2 Surveillance of Fire Protection Features and Eauioment
                    Test Procedure, Data Gathering Panel 13. Completed February 6.
.
                    1997.
a.
              -
Insoection Scone (64704)
                    PT/0/A/4400/01A, Revision Change 0 Retype 32. Exterior Fire
The inspectors reviewed the following completed surveillance and test
                    Protection Functional Capacity Test. Completed January 29, 1996.
procedures:
              -
-
                    PT/0/A/4400/01S, Revision Change 0 Retype 25. Exterior Fire
IP/0/A/3350/13. Revision Change 0 Retype 5. EFA System Detector
                    Protection System - Raw Water Yard (RY) Fire Protection Flow
Test Procedure, Data Gathering Panel 10.
                    (Underground) Periodic Test. Completed April 9.1996 and December
Completed January 20,
                    5, 1996.
1997.
            The frecuency of selected surveillance test procedures were also
-
              reviewec,
IP/0/A/3350/16. Revision Change 0 Retype 2. EFA System Detector
Test Procedure, Data Gathering Panel 13.
Completed February 6.
1997.
-
PT/0/A/4400/01A, Revision Change 0 Retype 32. Exterior Fire
Protection Functional Capacity Test.
Completed January 29, 1996.
-
PT/0/A/4400/01S, Revision Change 0 Retype 25. Exterior Fire
Protection System - Raw Water Yard (RY) Fire Protection Flow
(Underground) Periodic Test.
Completed April 9.1996 and December
5, 1996.
The frecuency of selected surveillance test procedures were also
reviewec,
i
i
                                                                                  Enclosure 2
Enclosure 2


                                      .   . _ .   __   . _ _ _ _ .   _           _ _ __
.
                                                                                          l
. _ .
    4
__
          .
. _ _ _ _ .
                                            34                                           l
_
                                                                                          l
_
      b. Observations and Find 1nas
_ __
        The completed fire protection surveillance tests reviewed by the
4
        inspectors had been appropriately completed and met the. acceptance             ;
.
        criteria. The test procedures were well written and met the fire                 !
34
          3rotection surveillance requirements of FSAR Chapter 16.9. Selected             ;
b.
          _icensee Commitments (SLC). The surveillance procedures for the                 ;
Observations and Find 1nas
        capacity tests on the fire pumps required test data for multiple points         j
The completed fire protection surveillance tests reviewed by the
        on the pump curve to be obtained. This data provided good verification           l
inspectors had been appropriately completed and met the. acceptance
        of the pump's performance.
criteria. The test procedures were well written and met the fire
        During the review of Surveillance PT/0/A4400/01A. the inspectors noted           l
3rotection surveillance requirements of FSAR Chapter 16.9. Selected
        that the October 1995 surveillance test indicated that the water flow
;
        through the piping system would not deliver adequate fire flows This
_icensee Commitments (SLC). The surveillance procedures for the
        test is conducted every three years and measures the flow of water               ;
capacity tests on the fire pumps required test data for multiple points
        through various sections of piping to determine if the system will               '
j
        provide an adequate flow path from the fire pumps to the various                 i
on the pump curve to be obtained.
        sprinkler and hose stations located in the plant to meet the required           l
This data provided good verification
        design head 3ressure and volume requirements.       Following the October
of the pump's performance.
        1995 test, t1e system was extensively flushed and retested in April             i
During the review of Surveillance PT/0/A4400/01A. the inspectors noted
        1996. This test found that the system remained deficient. The flow
that the October 1995 surveillance test indicated that the water flow
        tests were performed by isolating the normal loop piping such that the
through the piping system would not deliver adequate fire flows
  .      flow tests were through a single pipe. The system would provide the
This
        required design flow rates as long as the loop flow paths were
test is conducted every three years and measures the flow of water
        maintained in service.                                                           ;
through various sections of piping to determine if the system will
        The licensee developed a major pipe cleaning and flushing project
'
        utilizing the " hydro-lase" process which was performed by station
provide an adequate flow path from the fire pumps to the various
        personnel working under the supervision and coordination of a vendor
i
        specialist. During the pipe cleaning activities several automatic
sprinkler and hose stations located in the plant to meet the required
        sprinkler systems and hose stations were required to be removed from
l
        service. The licensee coordinated this work to require a minim;m number         ;
design head 3ressure and volume requirements.
        of systems to be inoperable at any one time. Appropriate compensatory           l
Following the October
        actions, consisting of a fire watch with backup fire suppression, were           ;
1995 test, t1e system was extensively flushed and retested in April
        provided as remedial actions while the required fire suppression systems         '
i
        were inoperable. Based on the review of the work activities and
1996. This test found that the system remained deficient.
        interviews with the plant staff, the inspectors concluded that good
The flow
        coordination and oversight of these activities were provided. Following
tests were performed by isolating the normal loop piping such that the
        completion of the pipe cleaning activities the underground piping was
flow tests were through a single pipe.
        retested in December,1996 and was found to be capable of delivering the
The system would provide the
        required fire flow.
.
        The surveillance requirements for the fire protection systems were
required design flow rates as long as the loop flow paths were
        contained in FSAR Chapter 16.9. The results of the inspector's review
maintained in service.
I       of these features is located in Section F3.
;
The licensee developed a major pipe cleaning and flushing project
utilizing the " hydro-lase" process which was performed by station
personnel working under the supervision and coordination of a vendor
specialist.
During the pipe cleaning activities several automatic
sprinkler systems and hose stations were required to be removed from
service.
The licensee coordinated this work to require a minim;m number
of systems to be inoperable at any one time.
Appropriate compensatory
actions, consisting of a fire watch with backup fire suppression, were
;
provided as remedial actions while the required fire suppression systems
'
were inoperable.
Based on the review of the work activities and
interviews with the plant staff, the inspectors concluded that good
coordination and oversight of these activities were provided.
Following
completion of the pipe cleaning activities the underground piping was
retested in December,1996 and was found to be capable of delivering the
required fire flow.
The surveillance requirements for the fire protection systems were
contained in FSAR Chapter 16.9.
The results of the inspector's review
I
of these features is located in Section F3.
l
l
      c. Conclusions
l
l
        Good surveillance and test procedures were provided for the fire
c.
        protection systems and features. Procedure implementation was
Conclusions
                                                                    Enclosure 2
Good surveillance and test procedures were provided for the fire
protection systems and features.
Procedure implementation was
Enclosure 2
!
!
                                                                                          l
                                                                                          1


    _     .     _     .   ._ _ __         - __   . ._   _-   ___           _         _.__.
_
      '
.
o
_
                .
.
                                                  35
._ _ __
              effective. The coordination of the fire protection water piping
- __
              cleaning project was excellent.
.
        F3   Fire Protection Procedures and Documentation
._
        a.     Insoection Scooe (64704)
_-
              The inspectors reviewed the following procedures for compliance with the
___
              NRC requirements and guidelines:
_
              -
_.__.
                      Nuclear Station Directive 112. Revision 0. Fire Brigade
I
                      Organization. Training and Responsibilities
'
              -
o
                      Site Directive 2.12.5, Revision 3. Control of Combustible
.
                      Materials Within the Protected Area
35
              -
effective. The coordination of the fire protection water piping
                      Site Directive 2.12.6. Revision 3. Fire Protection. Detection and
cleaning project was excellent.
                      Barrier Impairment Reporting
F3
              -
Fire Protection Procedures and Documentation
                      Site Directive 2.12.7. Revision 4. Fire Protection / Detection             !
a.
!                    Remedial Actions
Insoection Scooe (64704)
The inspectors reviewed the following procedures for compliance with the
NRC requirements and guidelines:
-
Nuclear Station Directive 112. Revision 0. Fire Brigade
Organization. Training and Responsibilities
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Site Directive 2.12.5, Revision 3. Control of Combustible
Materials Within the Protected Area
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Site Directive 2.12.6. Revision 3. Fire Protection. Detection and
Barrier Impairment Reporting
-
Site Directive 2.12.7. Revision 4. Fire Protection / Detection
!
Remedial Actions
!.
!.
              -
-
                      Site Directive 3.3.9. Revision 1. Hot Work Authorization
Site Directive 3.3.9. Revision 1. Hot Work Authorization
:             -
:
                      FSAR Chapter 16.9. (Revision dated 1/30/96). Auxiliary Systems
-
                      (Fire Protection Systems)
FSAR Chapter 16.9. (Revision dated 1/30/96). Auxiliary Systems
              -
(Fire Protection Systems)
                      Prefire Plans. Revision 6. Catawba Prefire Plans 6.1d Procedures
-
              Plant tours were also performed to assess procedure compliance.
Prefire Plans. Revision 6. Catawba Prefire Plans 6.1d Procedures
        b.   Observations and Findinas
Plant tours were also performed to assess procedure compliance.
              The above procedures were the principle procedures issued to implement
b.
              the facility's fire protection program. These procedures contained the
Observations and Findinas
              requirements for program administration. controls over combustibles and
The above procedures were the principle procedures issued to implement
i             ignition sources, fire brigade organization and training, and
the facility's fire protection program.
              o)erability requirements for the fire protection systems and features.
These procedures contained the
requirements for program administration. controls over combustibles and
i
ignition sources, fire brigade organization and training, and
o)erability requirements for the fire protection systems and features.
,
,
              T1e procedures were well written and met the licensee's commitments to
T1e procedures were well written and met the licensee's commitments to
!
!
              the NRC.
the NRC.
              The inspectors performed plant tours a"d noted that, even though the               l
The inspectors performed plant tours a"d noted that, even though the
              plant was in a refueling outage, implementation of the site's fire                 !
plant was in a refueling outage, implementation of the site's fire
l             prevention program for the control of ignition sources, transient                 ;
l
l             combustibles, and general housekeeping was good.         The accumulation of       j
prevention program for the control of ignition sources, transient
l
combustibles, and general housekeeping was good.
The accumulation of
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transient combustible materials and the number of maintenance activities
'
t
t
              transient combustible materials and the number of maintenance activities          '
in process due to the refueling outage were-more than anticipated during
              in process due to the refueling outage were-more than anticipated during
normal plant operations.
              normal plant operations. However, appropriate fire prevention controls
However, appropriate fire prevention controls
              were being applied to these activities.
were being applied to these activities.
                                                                                                !
Enclosure 2
                                                                          Enclosure 2
i
                                                                                                i
(
(


          .   ._                 . ___ _.             . ._ . _ . _ ._       __
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._
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___ _.
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._ . _ .
_ ._
__
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    ,
,
                  .
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                                                36
36
            FSAR Chapter 16.9. Selected Licensee Commitments. Auxiliary Systems
FSAR Chapter 16.9. Selected Licensee Commitments. Auxiliary Systems
              (Fire Protection Systems) provides the operability and surveillance
(Fire Protection Systems) provides the operability and surveillance
            requirements for the fire protection systems and components. The
requirements for the fire protection systems and components.
            inspectors compared these requirements to the requirements which were
The
            formerly in the TS. These requirements remained essentially the same,
inspectors compared these requirements to the requirements which were
            except for the following testing frequency changes: fire detectors.
formerly in the TS. These requirements remained essentially the same,
            from monthly to annually; fire protection valve alignments, from monthly
except for the following testing frequency changes:
:           to quarterly; and hose station inspection, from monthly to quarterly.
fire detectors.
            The licensee had recently changed these surveillance inspection
from monthly to annually; fire protection valve alignments, from monthly
:
to quarterly; and hose station inspection, from monthly to quarterly.
The licensee had recently changed these surveillance inspection
frequencies based on satisfactory results from performance based
,
,
            frequencies based on satisfactory results from performance based
l
l            evaluat wis of these systems. The inspectors verified that appropriate   ,
evaluat wis of these systems. The inspectors verified that appropriate
l           10 CFR 50.59 safety evaluations had been performed for these revisions.   l
l
            The trending data on the performance based surveillance inspections were !
10 CFR 50.59 safety evaluations had been performed for these revisions.
            reviewed and indicated that the reliability of these systems was greater l
,
            than 99 percent. This substantiated the changes made to the             !
The trending data on the performance based surveillance inspections were
            surveillance frequency requirements. The operability requirements in
reviewed and indicated that the reliability of these systems was greater
            the SLC were adequate. However, the water supply and fire detection
than 99 percent.
            systems were the only systems which had time limits established for
This substantiated the changes made to the
            restoring inoperable components to operable status. This issue is being
!
            evaluated further by the NRC and is identified as an Inspector Followup
surveillance frequency requirements. The operability requirements in
            Item pending completion of this review. IFI 50-413.414/97-07-06: Time
the SLC were adequate.
            Limits for Restoration of Inoperable Fire Protection Components.
However, the water supply and fire detection
  .
systems were the only systems which had time limits established for
            The prefire plans reviewed by the inspectors were found to be
restoring inoperable components to operable status. This issue is being
            satisfactory. A minor modification was in process to relocate and
evaluated further by the NRC and is identified as an Inspector Followup
            remove some of the fire extinguishers presently installed within the     .
Item pending completion of this review. IFI 50-413.414/97-07-06: Time
            plant. Also, a standard fire protection water supply system was         I
Limits for Restoration of Inoperable Fire Protection Components.
            scheduled to be installed by late 1991 for the nuclear service water     '
.
            intake pumping structure. The prefire plans were scheduled to be
The prefire plans reviewed by the inspectors were found to be
            revised upon completion of these modifications. In the interim.
satisfactory.
            controlled copies of the prefire plans had been marked to indicate the
A minor modification was in process to relocate and
            plant changes as they were completed for each plant area.
remove some of the fire extinguishers presently installed within the
        c.   Conclusions
.
            The fire protection program implementing procedures were good and met
plant. Also, a standard fire protection water supply system was
            licensee and NRC requirements. Implementation of procedures for the
scheduled to be installed by late 1991 for the nuclear service water
            control of ignition sources, transient combustibles, and general
'
            housekeeping was good. An issue regarding time limits for restoration
intake pumping structure.
            of inoperable fire protection components will be reviewed further by the
The prefire plans were scheduled to be
            NRC.
revised upon completion of these modifications.
        F5   Fire Protection Staff Training and Qualification
In the interim.
        a.   Inspection Scope (64704)
controlled copies of the prefire plans had been marked to indicate the
            The inspectors reviewed the fire brigade organization and training
plant changes as they were completed for each plant area.
            program for compliance with the NRC guidelines and requirements.
c.
Conclusions
The fire protection program implementing procedures were good and met
licensee and NRC requirements.
Implementation of procedures for the
control of ignition sources, transient combustibles, and general
housekeeping was good. An issue regarding time limits for restoration
of inoperable fire protection components will be reviewed further by the
NRC.
F5
Fire Protection Staff Training and Qualification
a.
Inspection Scope (64704)
The inspectors reviewed the fire brigade organization and training
program for compliance with the NRC guidelines and requirements.
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:
I                                                                   Enclosure 2
I
Enclosure 2


    -     -     -   ---           -     -         _.   - . -   - -.       --             . . . .-
-
              .
-
        .
-
                          .
---
!                                                               37
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37
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l                b.    Observations and Findinas
[                                                                                                      :
j                        The organization and training requirements for the 31 ant fire brigade
                        were established by Nuclear Station Directive 112. Revision 0. Fire            i
                        Brigade Organization. Training and Res]onsibilities. The fire brigade          I
                        for each shift was composed of a fire arigade leader and at least four
j                        brigade members from operations and approximately five members from
                        maintenance.    The fire brigade leeder was a senior reactor o]erator          i
                          (SRO) and was normally one of the unit shift supervisors. T1e other
                        members from Operations were non-licensed plant operators. One of the          i
!                        fire brigade members was normally assigned the duties of fire brigade
                        safety officer to provide technical and administrative assistance to the
                        fire brigade leader and to hel) cssure the safe performance of each fire
l                        brigade member by checking eac1 member for appropriate dress out prior
l                        to entering the fire area, maintaining records of each fire brigade            ,
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                        exposure to fire or radiatinn hazards, use of self contained breathing        l
b.
                        apparatus, and reviewing the prefire plans during the emergency for            '
Observations and Findinas
                        assurance that appropriate measures are being followed for compliance
[
l          '
j
                        with applicable safety and fire hazards in the area. Assignment of a
The organization and training requirements for the 31 ant fire brigade
l                       fire brigade safety officer was identified as a program strength.
were established by Nuclear Station Directive 112. Revision 0. Fire
i
Brigade Organization. Training and Res]onsibilities. The fire brigade
I
for each shift was composed of a fire arigade leader and at least four
j
brigade members from operations and approximately five members from
maintenance.
The fire brigade leeder was a senior reactor o]erator
(SRO) and was normally one of the unit shift supervisors. T1e other
members from Operations were non-licensed plant operators. One of the
i
!
fire brigade members was normally assigned the duties of fire brigade
safety officer to provide technical and administrative assistance to the
fire brigade leader and to hel) cssure the safe performance of each fire
l
brigade member by checking eac1 member for appropriate dress out prior
to entering the fire area, maintaining records of each fire brigade
l
l
                        Each fire brigade member was required to receive initial, quarterly and
,
      .
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                        annual fire fighting related training and to satisfactorily complete an
exposure to fire or radiatinn hazards, use of self contained breathing
                        annual medical evaluation and certification for participation in fire
apparatus, and reviewing the prefire plans during the emergency for
                        brigade fire fighting activities. In addition each member was required
'
i                        to participate in at least two drills per year.
assurance that appropriate measures are being followed for compliance
l
with applicable safety and fire hazards in the area. Assignment of a
'
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fire brigade safety officer was identified as a program strength.
l
Each fire brigade member was required to receive initial, quarterly and
annual fire fighting related training and to satisfactorily complete an
.
.
                        As of the date of this inspection, there were a total of 34 operations
annual medical evaluation and certification for participation in fire
                        trained fire brigade leaders and 73 operations personnel and 29
brigade fire fighting activities.
                        maintenance personnel on the plant's fire brigade. Approximately 6 fire
In addition each member was required
                        brigade leaders.12 operations fire brigade members and 5 mintenance
i
                        fire brigade members were assigned to each of the five operations crews.
to participate in at least two drills per year.
                        This was a sufficient number of personnel to meet the facilities fire
                        brigade procedure requirements for one team leader and nine members per
l                        shift.
                        The inspectors reviewed the training and medical records for the fire
                        brigade members and verified that the training and medical records were        I
                        up to date. The facility utilized off-site qualified state certified
                        fire brigade training instructors and a state fire training facility to
                        perform the annual fire brigade training and practical fire training
                                                                                                        ,
                                                                                                        i
                        scenarios.
                        During this inspection, the inspectors witnessed a fire brigade drill
                        involving a simulated fire in an electrical motor for a component
                        cooling pump located on the 560 foot elevation of the auxiliary
                        building. The response of the fire brigade to the simulated fire was
;                        excellent. The brigade leader's direction and fire brigade members'
  i
                        performance, especially the safety officer, were outstanding. A
.
.
!                                                                                 Enclosure 2
As of the date of this inspection, there were a total of 34 operations
trained fire brigade leaders and 73 operations personnel and 29
maintenance personnel on the plant's fire brigade. Approximately 6 fire
brigade leaders.12 operations fire brigade members and 5 mintenance
fire brigade members were assigned to each of the five operations crews.
This was a sufficient number of personnel to meet the facilities fire
brigade procedure requirements for one team leader and nine members per
l
shift.
The inspectors reviewed the training and medical records for the fire
brigade members and verified that the training and medical records were
up to date.
The facility utilized off-site qualified state certified
fire brigade training instructors and a state fire training facility to
perform the annual fire brigade training and practical fire training
,
i
scenarios.
During this inspection, the inspectors witnessed a fire brigade drill
involving a simulated fire in an electrical motor for a component
cooling pump located on the 560 foot elevation of the auxiliary
building.
The response of the fire brigade to the simulated fire was
;
excellent. The brigade leader's direction and fire brigade members'
i
performance, especially the safety officer, were outstanding.
A
.
!
Enclosure 2
,
,
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                                  _ _
_
      '
_
  , ,
            .
l                                              38
            critique to discuss the brigade performance and future enhancements was
'
'
,           held following the drill.
,
        c. Conclusions
,
            The fire brigade organization and training met the requirements of the
.
            site procedures. Performance by the fire brigade during a drill was
l
            excellent. The use of the fire brigade safety officer position during
38
            fire emergencies was identified as a program strength.
critique to discuss the brigade performance and future enhancements was
        F6 Fire Protection Organization and Administration
'
                                                                                    i
held following the drill.
        a. Insoection Scooe (64704)
,
                                                                                    ]
c.
            The licensee's managemerit and administration of the facilities fire     l
Conclusions
            protection program were reviewed for compliance with the commitments to
The fire brigade organization and training met the requirements of the
            the NRC and to current guidelines.                                       )
site procedures.
        b. Observations and Findinas
Performance by the fire brigade during a drill was
            The Civil. Electrical. Reactor. Nuclear Engineering Manager was assigned
excellent.
            the responsibility for implementing the facility's fire protection
The use of the fire brigade safety officer position during
,.          program. An engineer was assigned the task of coordinating the entire
fire emergencies was identified as a program strength.
            fire 3rotection program and for coordinating the maintenance,
F6
            opera)ility and modifications on the fire suppression systems, fire
Fire Protection Organization and Administration
            barriers, and fire barrier penetrations. Another engineer was           i
i
            responsible for coordinating the maintenance, o)erability and           !
a.
            modifications on the fire detection systems. T1e Manager of Safety       l
Insoection Scooe (64704)
            Assurance was responsible for providing appropriate training for the     i
]
            facility fire brigade and for providing guidance and support in the     '
The licensee's managemerit and administration of the facilities fire
            implementation of the facility's fire protection program. Support on
protection program were reviewed for compliance with the commitments to
            generic fire 3rotection issues was provided to the site by an engineer
the NRC and to current guidelines.
            assigned to t7e Corporate Nuclear Engineering Division.
b.
            A corporate Fire Protection Business Excellence Steering Team (BEST).
Observations and Findinas
            composed of representatives from each of the three Duke nuclear plants
The Civil. Electrical. Reactor. Nuclear Engineering Manager was assigned
            and the corporate staff, was meeting monthly to discuss fire protection
the responsibility for implementing the facility's fire protection
            issues and im)rovements needed to enhance the fire protection program at
program. An engineer was assigned the task of coordinating the entire
            each site. T1e inspectors reviewed the minutes for the first three
,.
            meetings in 1997 and noted a number of issues were under consideration
fire 3rotection program and for coordinating the maintenance,
            which, if im)lemented should improve the overall fire protection
opera)ility and modifications on the fire suppression systems, fire
            program at t1e Duke facilities. The inspector concluded that these
barriers, and fire barrier penetrations.
            meetings were a positive element of the facility's fire protection
Another engineer was
            program.
i
        c. Conclusions
responsible for coordinating the maintenance, o)erability and
modifications on the fire detection systems.
T1e Manager of Safety
Assurance was responsible for providing appropriate training for the
facility fire brigade and for providing guidance and support in the
'
implementation of the facility's fire protection program.
Support on
generic fire 3rotection issues was provided to the site by an engineer
assigned to t7e Corporate Nuclear Engineering Division.
A corporate Fire Protection Business Excellence Steering Team (BEST).
composed of representatives from each of the three Duke nuclear plants
and the corporate staff, was meeting monthly to discuss fire protection
issues and im)rovements needed to enhance the fire protection program at
each site.
T1e inspectors reviewed the minutes for the first three
meetings in 1997 and noted a number of issues were under consideration
which, if im)lemented should improve the overall fire protection
program at t1e Duke facilities.
The inspector concluded that these
meetings were a positive element of the facility's fire protection
program.
c.
Conclusions
Strong coordination and oversight were provided over the facility's fire
-
-
            Strong coordination and oversight were provided over the facility's fire
protection program.
            protection program. The Fire Protection BEST was a positive factor in
The Fire Protection BEST was a positive factor in
                                                                    Enclosure 2
Enclosure 2
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                              --           .     . .   .   .   - _ _ - -- - -           _ . _ - .
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                                                  39
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.
- _ _ - -- - -
_ . _ - .
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.
39
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the identification of potential problems and in the development and
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              the identification of potential problems and in the development and
implementation of enhancements to the fire protection program.
              implementation of enhancements to the fire protection program.
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          F7 Quality Assurance in Fire Protection Activities
F7
Quality Assurance in Fire Protection Activities
!
!
l          a.  Insoection Scooe (64704)
              The following audit report was reviewed:
              -
                      Audit SA-95-24(CN)(RA). Triennial Fire Protection Audit conducted
                      May 15 through June 8, 1995
          b. Observations and Findinas
              Audit SA-95-24(CN)(RA) was a triennial 0A audit of the facilities' fire
              protection program. The licensee informed the inspectors that this was
              the only comprehensive audit of the fire protection program performed
              since Duke's December 18, 1991, request to use performance based
              criteria for establishing auoit frequencies was approved by the NRC.'s
              letter dated May 7. 1992. Previously, the TS had required annual,
              biannual and triennial audits of the fire protection program.          However,
              based on the licensee's assessment of good fire protection performance.
  .          only this one triennial audit had been performed at Catawba in recent
              years.
              TS 6.5.2.9 identified a number of site audits which were performed under
              the cognizance of the Nuclear Safety Review Board. The licensee's
              December 18, 1991, letter indicated that the audit frequency for all of
              these audits were deleted from the TS. and the OA Topical report was to
              be revised to indicate that the " audits of selected aspects of
              operational phase activities are performed with a frequency commensurate
              with safety significance and in such a manner as to assure that an audit
              of all safety related functions is completed within a period of two
              years." The OA topical report was revised, but only requires an audit
              of all "0A Condition 1 functions" to be completed within a period of two
              years. Many of the audit items listed by TS Section 6.5.2.9 are
              classified as OA Condition 2 or 3 functions. The specified time for
              these audits are not listed in the OA topical report. The inconsistency
              of not providing a specified frequency for Condition 2 and 3 functions
              is being further reviewed by the NRC and is identified as Inspector
              Follow-up Item pending completion of this review. 50-413.414/97-07-07:
              Audit Frequency Requirements for Activities other than OA Condition 1
              Functions.
              The inspectors reviewed the audit findings from the 1995 OA report and
              the corrective actions taken on the identified discrepancies. The
              report indicated that a comprehensive audit had been performed with nine
              findings identified. The corrective action on each finding had been
              completed in a timely manner.
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l                                                                           Enclosure 2
a.
Insoection Scooe (64704)
The following audit report was reviewed:
-
Audit SA-95-24(CN)(RA). Triennial Fire Protection Audit conducted
May 15 through June 8, 1995
b.
Observations and Findinas
Audit SA-95-24(CN)(RA) was a triennial 0A audit of the facilities' fire
protection program.
The licensee informed the inspectors that this was
the only comprehensive audit of the fire protection program performed
since Duke's December 18, 1991, request to use performance based
criteria for establishing auoit frequencies was approved by the NRC.'s
letter dated May 7. 1992.
Previously, the TS had required annual,
biannual and triennial audits of the fire protection program.
However,
based on the licensee's assessment of good fire protection performance.
only this one triennial audit had been performed at Catawba in recent
.
years.
TS 6.5.2.9 identified a number of site audits which were performed under
the cognizance of the Nuclear Safety Review Board.
The licensee's
December 18, 1991, letter indicated that the audit frequency for all of
these audits were deleted from the TS. and the OA Topical report was to
be revised to indicate that the " audits of selected aspects of
operational phase activities are performed with a frequency commensurate
with safety significance and in such a manner as to assure that an audit
of all safety related functions is completed within a period of two
years." The OA topical report was revised, but only requires an audit
of all "0A Condition 1 functions" to be completed within a period of two
years. Many of the audit items listed by TS Section 6.5.2.9 are
classified as OA Condition 2 or 3 functions.
The specified time for
these audits are not listed in the OA topical report. The inconsistency
of not providing a specified frequency for Condition 2 and 3 functions
is being further reviewed by the NRC and is identified as Inspector
Follow-up Item pending completion of this review. 50-413.414/97-07-07:
Audit Frequency Requirements for Activities other than OA Condition 1
Functions.
The inspectors reviewed the audit findings from the 1995 OA report and
the corrective actions taken on the identified discrepancies. The
report indicated that a comprehensive audit had been performed with nine
findings identified.
The corrective action on each finding had been
completed in a timely manner.
l
l
Enclosure 2


                                                                                          k 2.m
k
                                                                                                  I
2.m
  s .. '
'
                  .
s ..
                                                    40
.
          c.     Conclusions
40
                The 1995 audit and assessment of the facility's fire protection program
c.
                was comprehensive and appropriate corrective action was promptly taken
Conclusions
                to resolve identified issues. An issue regarding the control of 0A
The 1995 audit and assessment of the facility's fire protection program
                audit frequencies will be reviewed further by the NRC.
was comprehensive and appropriate corrective action was promptly taken
          F8     MiscellaneousFireProtectjonIssues
to resolve identified issues. An issue regarding the control of 0A
          F8.1 Fire Protection Related NRC Information Notices
audit frequencies will be reviewed further by the NRC.
                The inspector reviewed the licensee's evaluation for the following NRC           1
F8
                Information Notices (IN):                                                       '
MiscellaneousFireProtectjonIssues
                -
F8.1 Fire Protection Related NRC Information Notices
                        IN 92-18. Potential loss of Shutdown Capacity During a Control
The inspector reviewed the licensee's evaluation for the following NRC
                        Room Fire
Information Notices (IN):
                -
'
                        IN 92-28. Inadequate Fire Suppression System Testing
-
                -
IN 92-18. Potential loss of Shutdown Capacity During a Control
                        IN 93-41. One Hour Fire Endurance Tests Results For Thermal
Room Fire
                        Ceramics. 3M Company FS 195'and 3M Company E-50 Interam Fire             ,
-
                        Barrier Systems                                                         I
IN 92-28. Inadequate Fire Suppression System Testing
-
IN 93-41. One Hour Fire Endurance Tests Results For Thermal
Ceramics. 3M Company FS 195'and 3M Company E-50 Interam Fire
,
Barrier Systems
..
..
                -
-
                        IN 94-28. Potential Problems with Fire Barrier Penetration Seals
IN 94-28. Potential Problems with Fire Barrier Penetration Seals
                -
-
                        IN 9--31. Potential Failure of WILCO. LEXAN-Type HN-4-L. Fire Hose
IN 9--31. Potential Failure of WILCO. LEXAN-Type HN-4-L. Fire Hose
                        Nozzles
Nozzles
                -
-
                        IN 94-58. Reactor Coolant Pump Lube Oil Fire
IN 94-58. Reactor Coolant Pump Lube Oil Fire
                -
-
                        IN 95-36. Emergency Lighting
IN 95-36. Emergency Lighting
                The licensee's evaluations and corrective actions for these ins were
The licensee's evaluations and corrective actions for these ins were
                appropriate, except the evaluation documentation for some of the ins did
appropriate, except the evaluation documentation for some of the ins did
                not fully indicate the results of the evaluations which were actually
not fully indicate the results of the evaluations which were actually
                performed.
performed.
                                        V. Manaaement Meetinos
V. Manaaement Meetinos
          X1     Exit Meeting Summary
X1
          The inspectors ) resented the inspection results to members of licensee
Exit Meeting Summary
:         management at t1e conclusion of the inspection on April 30. 1997. On May 14
The inspectors ) resented the inspection results to members of licensee
;        a teleconference was held between Region II DRS management and licensee
:
          management representatives to discuss the violation included with this report.
management at t1e conclusion of the inspection on April 30. 1997.
l         The licensee acknowledged the findings presented. No proprietary information
On May 14
a teleconference was held between Region II DRS management and licensee
;
management representatives to discuss the violation included with this report.
l
The licensee acknowledged the findings presented.
No proprietary information
was identified.
t
t
          was identified.                                                .
.
                                                                        Enclosure 2
Enclosure 2
i
i


                  - - . .       _.   _ . _ _ . _ _ _         - _ . . . _ _ _ _ - . _ . -
- - . .
                                                                                            _ _ . _ _ . _ _ _ _ - .
_.
_ . _ _ . _ _ _
- _
. . . _ _ _ _ - . _ .
_ _ . _ _ . _ _ _
_ - .
-
,
l
l
"
, , - . .
,
,
:
-
l
41
l
i
l
l
l
'
PARTIAL LIST OF PERSONS CONTACTED
Licensee
Bhatnager,
A., Operations Superintendent
Birch. M., Safety Assurance Manager
Christopher. S. , Emergency Planning Supervisor
.
'
l
l
        "
Copp. S Nuclear Regulatory Affairs Manager
,,-..                                                                                                             ,
Coy. S., Radiation Protection Manager
                                                                                                                      :
'
                  -
i
Forbes. J.,
Engineering Manager
'
Giles, R.
Work Control Inservice Inspection Coordination
,
Harrall. T.
Instrument and Electrical Maintenance Superintendent
'
:
:
l                                                          41
Kelly. C.. Maintenance Manager
l                                                                                                                    i
!
Kimball. D., Safety Review Group Manager
!
Kitlan. M., Regulatory Compliance Manager
'
Kulla
D.
Civil Engineering Supervisor
McCollum
W., Catawba Site Vice-President
i
Nicholson. K., Compliance Specialist
J
l
l
                                                                                                                      l
Peterson. G., Station Manager
l.
Propst. R., Chemistry Manager
l
l
Purser, M.. Senior Engineer
,
l
l
                                                                                                                      '
Robinson
                                          PARTIAL LIST OF PERSONS CONTACTED
G., Work Control Execution Support
          Licensee
l
          Bhatnager, A., Operations Superintendent
Rogers
          Birch. M., Safety Assurance Manager                                                                       .
D., Mechanical Maintenance Manager
          Christopher. S. , Emergency Planning Supervisor                                                            '
i
l          Copp. S Nuclear Regulatory Affairs Manager
Tower, D., Compliance Engineer
'
'
          Coy. S., Radiation Protection Manager                                                                      i
i
          Forbes. J., Engineering Manager                                                                            '
          Giles, R. Work Control Inservice Inspection Coordination                                                  ,
          Harrall. T. Instrument and Electrical Maintenance Superintendent                                          '
:          Kelly. C.. Maintenance Manager
!          Kimball. D., Safety Review Group Manager
!          Kitlan. M., Regulatory Compliance Manager                                                                  '
          Kulla  D.      Civil Engineering Supervisor
          McCollum W., Catawba Site Vice-President
          Nicholson. K., Compliance Specialist
i
                                                                                                                      J
l          Peterson. G., Station Manager
l.        Propst. R., Chemistry Manager
          Purser, M.. Senior Engineer
                                                                                                                      ,
l                                                                                                                    l
l          Robinson G., Work Control Execution Support
l        Rogers D., Mechanical Maintenance Manager                                                                  i
          Tower, D., Compliance Engineer                                                                            '
                                                                                                                      i
(
(
                                                                                                                      )
)
                                                                                                                      I
I
!
!
>
>
                                                                                                                      \
\\
                                                                                                                      l
l
                                                                                                                      1
1
                                                                                                                      l
,
                                                                                                                      l
Enclosure 2
                                                                                                                      l
l
                                                                                                                      ,
                                                                                          Enclosure 2
l
l
                                                                                                                      l
i
i                                                                                                                    j
j


              .-                           -         - - -           .   .-
.-
        '
-
    7..
- - -
                  .
.
                                                    42
.-
                                      INSPECTION PROCEDURES USED
'
          IP 37550:   Engineering
7..
          IP 37551:   Onsite Engineering
.
          IP 40500:   Effectiveness of Licensee Controls in Identifying, Resolving, and
42
                      Preventing Problems
INSPECTION PROCEDURES USED
IP 37550:
Engineering
IP 37551:
Onsite Engineering
IP 40500:
Effectiveness of Licensee Controls in Identifying, Resolving, and
Preventing Problems
IP 49001:
Inspection of Erosion / Corrosion Monitoring Programs
'
'
!
!
          IP 49001:   Inspection of Erosion / Corrosion Monitoring Programs
IP 61726:
          IP 61726:  Surveillance Observation
Surveillance Observation
          IP 62001:   Boric Acid Program Prevention Program
IP 62001:
          IP 62707:   Maintenance Observation
Boric Acid Program Prevention Program
IP 62707:
Maintenance Observation
IP 64704:
Fire Protection Program
,
,
'
'
          IP 64704:   Fire Protection Program
IP 71707:
          IP 71707:  Plant Operations
Plant Operations
l        IP 71750:   Plant Support Activities
IP 71750:
Plant Support Activities
l
IP 73753:
Inservice Inspection
'
'
          IP 73753:   Inservice Inspection
IP 83750:
          IP 83750:  Occupational Radiation Exposure
Occupational Radiation Exposure
l         IP 84750:   Radioactive Waste Treatment and Effluent and Environmental
l
                      Monitoring
IP 84750:
          IP 92901:   Followup - Operations
Radioactive Waste Treatment and Effluent and Environmental
          IP 92902:   Followup - Maintenance
Monitoring
          IP 92903:   Followup - Engineering
IP 92901:
                                ITEMS OPENED, CLOSED, AND DISCUSSED
Followup - Operations
  .
IP 92902:
          Opened
Followup - Maintenance
          50-414/97-07-01           VIO   OPEN             Inadequate Procedure Resulting in
IP 92903:
                                                          Loss of Spent Fuel Pool Cooling with
Followup - Engineering
                                                          Core Off-loaded. (Section 01.1)
ITEMS OPENED, CLOSED, AND DISCUSSED
          50-413,414/97-0? 32       1FI   OPEN           Boron Dilution Mitigation System
.
                                                          Reliability Resolution. (Section
Opened
                                                          01.4)
50-414/97-07-01
          50-413.414/97-07-03       IFI   OPEN           Review Corrective Actions For
VIO
                                                          Storage and Handling Assessment
OPEN
                                                          Findings. (Section M1.2)
Inadequate Procedure Resulting in
          50-413,414/97-07-04       NCV   OPEN           Failure to Source Check Survey
Loss of Spent Fuel Pool Cooling with
                                                          Instruments as required by licensee
Core Off-loaded. (Section 01.1)
                                                          procedure. (Section R1.1)
50-413,414/97-0? 32
          50-413.414/97-07-05       VIO   OPEN           Failure to Repair Degraded Suction
1FI
                                                          Screen Filters for Fire Pumps in a
OPEN
                                                          Timely Manner. (Section F2.1)
Boron Dilution Mitigation System
          50-413,414/97-07-06       IFI   OPEN           Time Limits for Restoration of
Reliability Resolution. (Section
01.4)
50-413.414/97-07-03
IFI
OPEN
Review Corrective Actions For
Storage and Handling Assessment
Findings. (Section M1.2)
50-413,414/97-07-04
NCV
OPEN
Failure to Source Check Survey
Instruments as required by licensee
procedure. (Section R1.1)
50-413.414/97-07-05
VIO
OPEN
Failure to Repair Degraded Suction
Screen Filters for Fire Pumps in a
Timely Manner. (Section F2.1)
50-413,414/97-07-06
IFI
OPEN
Time Limits for Restoration of
Inoperable Fire Protection
,
,
                                                          Inoperable Fire Protection
Components. (Section F.3)
                                                          Components. (Section F.3)
l
l
j                                                                               Enclosure 2
j
Enclosure 2


        _..         _ _   _ . _ _ . _ _ _ .           . _ . _ . . . -       . . - . - _ _ _ _ . . _ .       .   _ . _ _ . . . _ _ _
_..
_
_
_
. _ _ . _ _ _ .
. _ . _ . . . -
. . - . - _ _ _ _ . . _ .
.
_ . _ _ . . . _ _ _
:
:
    3..*
3..*
                    .
.
                                                              43
43
            50-413.414/97-07-07               IFI OPEN                   Audit Frequency Requirements for
50-413.414/97-07-07
                                                                          Activities other than OA Condition 1
IFI
                                                                          Functions. (Section F.7)                                       :
OPEN
            Closed
Audit Frequency Requirements for
            50-413.414/94-13-01               VIO CLOSED                 Failure to follow Procedure NSD 703
Activities other than OA Condition 1
                                                                          and Station Directive 34.0.5
Functions. (Section F.7)
                                                                          requirements. (Section 08.1)
:
l           50-413/95-07-01                   VIO CLOSED                 Inadequate Modification Procedure                               !
Closed
                                                                          Resulting in Loss of RHR. (Section                             ,
50-413.414/94-13-01
VIO
CLOSED
Failure to follow Procedure NSD 703
and Station Directive 34.0.5
requirements.
(Section 08.1)
l
50-413/95-07-01
VIO
CLOSED
Inadequate Modification Procedure
Resulting in Loss of RHR. (Section
i
i
                                                                          08.2)
,
            50-413.414/95-07-02             VIO   CLOSED                 Inadequate Valve Verification
08.2)
                                                                          Activities - Two Examples. (Section
50-413.414/95-07-02
                                                                          08.3)
VIO
            50-413.414/96-13-04             VIO   CLOSED                 Inadequate Design Controls (MSIV
CLOSED
                                                                          Solenoid Valves). Standby Shutdown
Inadequate Valve Verification
                                                                          System Makeup Pump Sizing
Activities - Two Examples. (Section
                                                                          Calculation (Section E8.1)
08.3)
  .
50-413.414/96-13-04
            50-413.414/92-01-06             DEV   CLOSED                 Breaker Coordination (Section E8.2)
VIO
            50-413.414/96-12-03             VIO   CLOSED                 Inadequate Design Controls For
CLOSED
                                                                          Ensuring Containment Crane Wall and
Inadequate Design Controls (MSIV
                                                                          Floor Drain Screens Implemented
Solenoid Valves). Standby Shutdown
                                                                          Design Requirements (Section E8.3)
System Makeup Pump Sizing
l                                                                                                         Enclosure 2
Calculation (Section E8.1)
      _           _                                   ,   _
50-413.414/92-01-06
DEV
CLOSED
Breaker Coordination (Section E8.2)
.
50-413.414/96-12-03
VIO
CLOSED
Inadequate Design Controls For
Ensuring Containment Crane Wall and
Floor Drain Screens Implemented
Design Requirements (Section E8.3)
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Enclosure 2
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_


I
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,
          '
'
      g..
g..
      6
6
                      .
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                                                    44
44
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l                                        LIST OF ACRONYMS USED
LIST OF ACRONYMS USED
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l
            ALARA -     As Low As Reasonably Achievable
ALARA -
            ANSI   -
As Low As Reasonably Achievable
                        American Nuclear Standards Institute
ANSI
            ASME -     American Society of Mechanical Engineers
-
American Nuclear Standards Institute
ASME -
American Society of Mechanical Engineers
BDMS -
Boron Dilution Mitigation System
,
,
'
'
            BDMS -      Boron Dilution Mitigation System
CA
            CA      -
-
                        Auxiliary Feedwater (system)
Auxiliary Feedwater (system)
            CHEC -     Designation for EPRI computer code
CHEC -
            CFR     -
Designation for EPRI computer code
                        Code of Federal Regulations
CFR
            DEV     -
-
                        Deviation
Code of Federal Regulations
            DG     -
DEV
                        Diesel Generator
-
            DPC     -
Deviation
                        Duke Power Company
DG
            EFA     -
-
                        Fire Detection System
Diesel Generator
            EPRI   -
DPC
                        Electric Power Research Institute
-
            ESS     -
Duke Power Company
                        Electric System Support
EFA
            FAC     -
-
                        Flow Accelerated Corrosion
Fire Detection System
            FME     -
EPRI
                        Foreign Material Exclusion
-
            FSAR -     Final Safety Analysis Report
Electric Power Research Institute
            FWST -     Refueling Water Storage Tank
ESS
              2
-
            ft   -
Electric System Support
                        Square Feet
FAC
            ft-lb -     foot-pounds (force)
-
            GL     -
Flow Accelerated Corrosion
                        Generic Letter
FME
    .      IFI     -
-
                        Inspector Followup Item
Foreign Material Exclusion
            IN     -
FSAR -
                        Information Notice
Final Safety Analysis Report
            IR     -
FWST -
                        Inspection Report
Refueling Water Storage Tank
            ISI     -
2
                        Inservice Inspection
ft
            MOV     -
-
                        Motor Operated Valve
Square Feet
            MSIV -     Main Steam Isolation Valve
ft-lb -
            NCV     -
foot-pounds (force)
                        Non Cited Violation
GL
            NDE     -
-
                        Nondestructive Examination
Generic Letter
            NI     -
IFI
                        Nuclear Safety Injection (system)
-
            NSD     -
Inspector Followup Item
                        Nuclear System Directive
.
            NSM     -
IN
                        Nuclear Station Modification
-
            NRC     -
Information Notice
                        Nuclear Regulatory Commission
IR
            OAC     -
-
                        Operator Aid Computer
Inspection Report
            PCE     -
ISI
                        Personnel Contamination Event
-
            PIP     -
Inservice Inspection
                        Problem Investigation Process
MOV
            PORV -     Power Operated Relief Valve
-
            psig -     Pounds Per Square Inch Gauge
Motor Operated Valve
            QA     -
MSIV -
                        Quality Assurance
Main Steam Isolation Valve
            RCA     -
NCV
                        Radiologically Controlled. Area
-
            RCP     -
Non Cited Violation
                        Reactor Coolant Pump
NDE
            RCS     -
-
                        Reactor Coolant System
Nondestructive Examination
            RHR     -
NI
                        Residual Heat Removal
-
            RP     -
Nuclear Safety Injection (system)
                        Radiation Protection
NSD
            rpm    -
-
                        revolutions per minute
Nuclear System Directive
            RWP     -
NSM
                        Radiation Work Permits
-
            SG     -
Nuclear Station Modification
                        Steam Generator
NRC
            SI     -
-
                        Safety Injection
Nuclear Regulatory Commission
l           SLC     -
OAC
                        Select Licensee Commitments
-
  '
Operator Aid Computer
                                                                Enclosure 2
PCE
                                                                            .
-
Personnel Contamination Event
PIP
-
Problem Investigation Process
PORV -
Power Operated Relief Valve
psig -
Pounds Per Square Inch Gauge
QA
-
Quality Assurance
RCA
-
Radiologically Controlled. Area
RCP
-
Reactor Coolant Pump
RCS
-
Reactor Coolant System
RHR
-
Residual Heat Removal
RP
-
Radiation Protection
revolutions per minute
rpm
-
RWP
-
Radiation Work Permits
SG
-
Steam Generator
SI
-
Safety Injection
l
SLC
-
Select Licensee Commitments
'
Enclosure 2
.


        *
*
    a.-
a.-
    s
s
                  .
.
                                              45
45
          SSS   -
SSS
                    Standby Shutdown System
-
          TEPR -   Top Equipment Problem Resolution
Standby Shutdown System
          TS   -
TEPR -
                    Technical Specifications
Top Equipment Problem Resolution
          UFSAR -   Updated Final Safety Analysis Report
TS
          VIO   -
-
                    Violation
Technical Specifications
          VN   -
UFSAR -
                    Variation Notice
Updated Final Safety Analysis Report
          WO   -
VIO
                    Work Order
-
  .
Violation
VN
-
Variation Notice
WO
-
Work Order
.
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                                                        Enclosure 2
Enclosure 2
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Latest revision as of 11:43, 11 December 2024

Insp Repts 50-413/97-07 & 50-414/97-07 on 970323-0426. Violations Noted.Major Areas Inspected:Licensee Operations, Maint,Engineering & Plant Support
ML20148F944
Person / Time
Site: Catawba  Duke Energy icon.png
Issue date: 05/23/1997
From:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML20148F917 List:
References
50-413-97-07, 50-413-97-7, 50-414-97-07, 50-414-97-7, NUDOCS 9706050102
Download: ML20148F944 (50)


See also: IR 05000413/1997007

Text

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U.S. NUCLEAR REGULATORY COMMISSION

REGION II

Docket Nos:

50-413, 50-414

License Nos:

NPF-35 NPF-52

Report Nos.:

50-413/97-07. 50-414/97-07

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Licensee:

Duke Power Company

Facility:

Catawba Nuclear Station Units 1 and 2

Location.

422 South Church Street

Charlotte. NC 28242

Dates:

March 23 - April 26,1997

Inspectors:

R. J. Freudenberger, Senior Resident Inspector

P. A. Balmain, Resident Inspector

R. L. Franovich. Resident Inspector

R. A. Gibbs, Resident Inspector (In Training)

.

J. L. Coley, Jr. . Reactor Inspector (Sections M2, E2.1)

D. B. Forbes, Radiation Specialist (Sections R1, R5, R7)

W. H. Miller, Jr.. Reactor Inspector (Sections 08.1, F2,

F3. FS, F6. F7 F8)

R. L. Moore, Reactor Inspector (Sections E2.2, E4.1, E8.1.

E8.2)

Approved by:

C. A. Casto, Chief

Reactor Projects Branch 1

Division of Reactor Projects

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Enclosure 2

9706050102 970523

PDR

ADOCK 05000413

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EXECUTIVE SUMMARY

Catawba Nucleer Station. Units 1 & 2

4

NRC Inspection Report 50-413/97-07. 50-414/97-07

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This integrated inspection included aspects of licensee operations.

maintenance, engineering, and plant support. The report covers a 6-week

period of resident ins)ection: in addition. it includes the results of

announced inspections ay regional reactor safety inspectors.

Operations

A Unit 2 loss of spent fuel pool cooling, which was caused by an

.

inadequate containment penetration test procedure, was identified as a

violation.

Other barriers that could have prevented the event included

increased emphasis on the importance of the system function during the

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pre-job brief and more diligent control board monitoring.

The

operator's performance in response to the event was appropriate.

The

Catawba Safety Review Group evaluation of the event was detailed and

identified substantive corrective actions. (Section 01.1)

Midloop Activities were well controlled.

Nevertheless, the process for

restoring equipment necessary for gravity flows to the core may not be

ensured by administrative controls. (Section 01.2)

.

The inspector concluded that selected initial conditions for the

.

compensatory action associated with the main control room pressure

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boundary were satisfied.

The inspector further concluded that operator

effectiveness in im)lementing this complex compensatory action was

challenged by lengtly initial conditions, and the practice of not

'

periodically reverifying required initial conditions. (Section 01.3)

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Problems encountered with the Boron Dilution Mitigation System during

.

the Unit 2 refueling outage were indicative of historically low

reliability and availability, which caused additional control room

operator workload to compensate for the system's low reliability.

(Section 01.4)

The inspector concluded that actions by operations and Radiation

.

Protection personnel in response to the radiation alarm in the fuel

handling building were good. However. foreign material exclusion

administrative controls were not properly im)lemented by personnel

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working in the fuel transfer canal area of t1e fuel handling building.

(Section 01.5)

!

A Unit 1 pressurizer )ower operated relief block valve control circuit

.

failure occurred whic1 is a potential repeat of a previous 1995 failure.

The licensee has planned appropriate actions to determine the cause of

the control circuit component failure. (Section 01.6)

Enclosure 2

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Maintenance

The inspector concluded that, in general, outage-related maintenance

.

activities were ap]ropriately conducted. Although multiple barriers to

minimizing the risc of human error during reactor coolant pump seal

maintenance were noted, the inspector was unaware of any human

performance problems associated with the work. (Section M1.1)

The licensee's resolution of long-standing elevated vibration levels

.

associated with the Unit 2B nuclear service water pump motor was very

good.

Deficiencies identified with a spare nuclear service water pump

motor, a previous motor failure, and findings identified by licensee

assessments of warehouse storage and handling practices raised questions

about control and storage of spare motors. The issue is identified as

an Inspector Followup Item and will be reviewed during a future

inspection. (Section M1.2)

Certification records for nondestructive examination (NDE) personnel,

weld examinations, and NDE examination procedures were in accordance

with Code requirements. (Section M2.1)

Review of the eddy current outage plan, equipment setup and acquisition

.

procedures, personnel and equipment certifications, and observation of

data acquisition activities revealed that required documentation was

available and complete, and data acquisition personnel were

-

knowledgeable of the eddy current examination process. (Section M2.2)

The licensee has implemented an effective program for the detection of

+

flow accelerated corrosion in components. This program is based on

recommendations found in recognized industry standards. (Section M2.3)

The maintenance / work control self-assessment programs effectively

.

identified areas for improvement and a]propriate corrective actions.

The self-assessments apparently contri)uted to improvement in the

performance of the Maintenance and Work Control organizations. (Section

M7.1)

Enaineerina

The licensee's actions to replace all control rod assemblies that had

.

evidence of tip cracking were appropriate. (Section El.1)

Documentation for the modification of the Unit 2 pressurizer manway was

satisfactory, and engineering considerations for the modification,

inspection, and cleaning of the pressurizer were very good. (Section

E2.1)

Design controls for Unit 2 outage modifications were consistent with

regulatory requirements. (Section E2.2)

Enclosure 2

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The motor shaft key way cracking in large high speed limitorque motor

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actuators at-Catawba was an example of good identification and

resolution of equipment problems using the Operating Experience Program.

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(Section E4.1)

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Plant Sucoort

The licensee was effectively maintaining controls for personnel

.

.

monitoring, control of radioactive material, radiological postings. and

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radiation area /high radiation area controls as required by 10 CFR Part 20. One Non-Cited Violation was identified for failure to source check

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survey instruments as required by licensee procedure. (Section R1.1)

The licensee was maintaining programs for controlling exposures As Low

[

.

As Reasonably Achievable and continued to be effective in controlling

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overall collective dose. (Section R1.2)

Radiation protection technicians and radiation workers were receiving an

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appropriate level of training to perform work activities involving

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radiation and/or radioactive material. (Section RS)

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The licensee was performing Quality Assurance Audits and effectively

.

assessing the radiation protection program as required by 10 CFR Part

.

20.1101 and completing corrective actions in a timely manner. (Section

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R7)

l.

The low number of open maintenance work orders and degraded fire

.

protection components, in conjunction with the good material condition

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of the fire protection components and fire brigade equipment, indicated

that, in general

appropriate em3hasis had been placed on the

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maintenance and operability of t1e fire protection equipment and

components. (Section F2.1)

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The work to repair the suction screens for the fire pumps' suction

. -

piping had been ooen since 1991 and was not complete.

The failure to.

complete this work in a timely manner was identified as a Violation.

(Section F2.1)

Good surveillance and test procedures were provided for the fire

.

protection systems and features with effective procedure implementation.

.The coordination of the fire protection water piping cleaning project

was excellent. (Section F2.2)

The fire protection program implementing procedures were good and met

!

.

licensee and NRC requirements.

Implementation of procedures for the

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control of. ignition sources, transient combustibles, and general

'

housekeeping was good. An issue regarding time limits for restoration

of inoperable fire protection components will be reviewed further by the

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NRC under an Inspector Followup Item.

(Section F3)

4

Enclosure 2

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The fire brigade organization and training met the requirements of the

.

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site procedures.

Performance by the fire brigade during a drill was

excellent. The use of the fire brigade safety officer position used

during fire emergencies was identified as a program strength. (Section

F5)

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Strong coordination and oversight were provided over the facility's fire

.

protection program.

The Fire Protection BEST was a positive force in

the identification of potential problems and in the development and

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implementation of enhancements to the fire protection program. (Section

F6)

,

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The 1995 audit and assessment of the facility's fire protection program

.

was comprehensive and appropriate corrective action was promptly taken

to reso:ve the identified issues. An issue regarding the control of OA

audit frequencies was identified as an Inspector Followup Item will be

reviewed further by the NRC. (Section F7)

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Enclosure 2

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Report Details

Summary of Plant Status

Unit 1 began the ]eriod operating at 100% power and operated at essentially

full power througacut the inspection period.

Unit 2 began the period in cold shutdown (Mode 5) in preparation for the End

of Cycle (EOC8) refueling outage. One scheduled period of reactor coolant

system reduced inventory /midloop began and completed on April 23.

Midloop was

entered to support the reactor coolant system vacuum refill evolution. At the

close of the inspection period the Unit had returned to cold shutdown (Mode 5)

and heatup activities in preparation for unit restart were beginning.

Review of Uodated Final Safety Analysis Reoort (UFSAR) Commitgents

While performing inspections discussed in this report, the inspectors reviewed

the applicable portions of the UFSAR that were related to the areas inspected.

The inspectors verified that the UFSAR wording was consistent with the

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observed plant practices, procedures, and/or parameters,

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I. Operations

01

Conduct of Operations

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01.1 Loss of Spent Fuel Pool Coolina

a. Insoection Scope (71707)

On April 8. Unit 2 was in a refueling outage with all of the fuel off-

loaded to the spent fuel pool.

The Operator Aid Computer was out of

'

service for replacement, and alignments for testing of containment

isolation valves in the component cooling water non-essential header

were in progress.

Inventory was inadvertently drained from the

component cooling water system over a seventy minute period. until the

low-low level setpoint in the component cooling water surge tanks was

reached. At this level, automatic isolation of the non-essential header

occurred. the drain path was isolated, and cooling flow to the spent

fuel pool heat exchanger and pump motor cooler was isolated.

0]erators

shutdown the pump to prevent overheating, initiated makeup to t1e

component cooling water surge tanks. and closely monitored spent fuel

pool temperature. Spent fuel pool temperature increased to a maximum of

108 F. within the TS limit. while operators determined the cause of the

loss of component cooling water inventory and returned the non-essential

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header to service.

!

As a result of the event, the licensee initiated Problem Investigation

Process (PIP) report 2-C97-1090 and initiated a root cause evaluation

that was performed by the Catawba Safety Review Group.

The inspector responded to the site upon notification of the loss of

spent fuel pool cooling: discussed the event with various personnel

Enclosure 2

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involved; reviewed PT/2/A/4200/01T, Containment Penetration Valve

Injection Water System Performance Test, approved 3/26/97: reviewed data

on component cooling water surge tank level spent fuel pool cooling

pump motor temperatures, and spent fuel pool temperature: and reviewed

the root cause evaluation documented in the referenced PIP.

b. Observations and Findinas

At the time of the loss of spent fuel pool cooling, approximately 19

-

hours were available prior to boiling in the spent fuel pool. Operators

methodically restored cooling within 1.5 hours5.787037e-5 days <br />0.00139 hours <br />8.267196e-6 weeks <br />1.9025e-6 months <br />, after identifying the

cause, assessing equipment condition, and realigning the component

.

cooling water system.

The licensee's root cause evaluation considered procedural adequacy.

o]erator performance, ad supervisory oversight of the evolution.

In

taese areas, problems were identified and appropriate corrective actions

were delineated.

Procedure PT/2/A/4200/01T, Containment Penetration Valve Injection Water

System Performance Test, included steps for the alignment of four

component cooling water containment penetrations that included valve

manipulation sequences that were incorrect. The incorrect sequences

.

caused drain paths to be aligned through the inside containment

penetration vent on all four penetrations. The licensee's evaluation

revealed that the Unit 1 procedure had similar errors. The errors

occurred during a process to convert engineering test procedures into

the operations procedure format.

Proposed corrective actions included a

formal validation of the technical adequacy of other procedures that

have been or were to be converted. This procedure inadequacy, which

caused the loss of spent fuel cooling constitutes a Violation (VIO) of

TS 6.8.1. Procedures and Programs, and is identified as VIO 50-414/97-

07-01:

Inadequate Procedure Resulting in Loss of Spent Fuel Pool

Cooling with Core Off-loaded.

The licensee's evaluation of operator performance concluded that the

equipment operator that performed the valve alignments appropriately

questioned the high flow rate from the vent valves as they were opened,

but failed to stop and contact su3ervision when this unexpected response

was obtained. Also, the control aoard operators were not timely in

their assessment of an observed increased rate of input to the

containment floor and equipment sump.

The inspector noted that the pre-job brief for performing the

containment Jenetration alignments was incomplete.

Personnel conducting

the pre-job arief did not emphasize that the component cooling water

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system was affected by the procedure and was being relied upon for

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Enclosure 2

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cooling the spent fuel pool with the core off-loaded.

Also, the control

room operators could have more diligently monitored this system, since

it was performing an important function, and identified the decreasing

level in the component cooling water surge tanks before automatic

actions occurred. Operations management had similar observations and

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took actions to imarove monitoring of systems performing important

functions during t1e remainder of the outage.

c. Conclusions

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The loss of spent fuel pool cooling was caused by an inadequate

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containment penetration test procedure.

Other barriers that could have

!

prevented the event included increased emphasis on the importance of the

system function during the pre-job brief and more diligent control board

monitoring.

The operator's performance in response to the event was

appropriate. The Catawba Safety Review Group evaluation of the event

was detailed and identified substantive corrective actions.

01.2 Preoarations for Midlooo

!

a. Insoection Scooe (71707)

l.

Near the conclusion of its refueling outage. Unit 2 entered midloo) on

!

April 23 for vacuum refill of the Reactor Coolant System (RCS). Tie

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inspector reviewed Generic Letter 88-17. Loss of Decay Heat Removal.

Catawba Nuclear Site Directive 3.1.30. Unit Shutdown Configuration

!

Control. Rev. 8. and the operating 3rocedures governing the RCS

draindown to midloop, operation wit 1 reduced RCS inventory, and vacuum

,

refill. The inspector conducted control room observations during the

draindown to midloop and portions of unit operation at midloop.

b. Observations and Findinos

The inspector verified that the requirements delineated in Catawba

Nuclear Site Directive 3.1.30 were satisfied.

Specifically, multiple

thermocouples were available for temperature monitoring; ultrasonics and

sightglass indications were available for level monitoring: vital power

was available from both offsite sources, as well as two emergency diesel

generators; necessary emergency core cooling equipment was either

operable or available: and the gravity flowpath criteria were satisfied

for midloop operation with low decay heat.

Just prior to reduced inventory operations, the inspector noticed that

valves 2ND-33. Residual Heat Removal (RHR) System Return to the

Refueling Water Storage Tank (FWST). 2FW-27A and 2FW-55B. RHR Pumps 2A

and 2B Suction from the FWST. were available as opposed to operable.

These valves are in the flowpaths of the three gravity feeds to the RCS.

The valves were tagged closed in support of RCS maintenance.

The

inspector questioned the a)proariateness of considering the associated

,

!

flowpaths available with tie RiR and FWST valves closed under a tagout.

Enclosure 2

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Normal makeup to the reactor coolant system via the chemical and volume

control system was available.

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The inspector inquired about the status of the RHR and FWST valves

during reduced inventory and midloo) operations and determined that.

although they were tagged closed, t1e Work Control Center filed the tags

,

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in a prominent location to facilitate equipment restoration in the event

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that these valves were needed to mitigate a loss of RHR.

The inspector reviewed Catawba Nuclear Site Directive 3.1.30 to

determine if administrative requirements were being met. The directive

stated that, for midloop operations with low decay heat load, two

available gravity flowpaths were required. The directive defines

l

"available" as "the status of a system, structure or component that is

'

in service or can be placed in service in a functional or operable state

by immediate manual or automatic actuation." The directive considers

actions taken by operators to clear tags acceptable for restoring

,

equipment to functional or operable status within a reasonable period of

time.

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The inspector raised a concern to the licensee that, while valves 2FW-

27A. 2FW-55B. and 2ND-33 could possibly be restored to service in a

reasonable period of time, other components that might be impacted by

.

the maintenance activity in progress might not be accounted for before

the gravity flowpath would be utilized.

Hence, points of compromised

'

system integrity, which could allow flow to be diverted from the RCS.

might be overlooked and either reduce the assumed flow to the RCS or

!

extend the amount of time needed to place the gravity flowpath in

service.

Although no such conditions were identified during the midloop

and vacuum refill evolutions, the licensee plans to evaluate Nuclear

Site Directive 3.1.30 to determine if changes are warranted prior to the

next refueling outage.

c. Conclusions

The inspector concluded that the draindown to midloop, midloop

operation, and vacuum refill were conducted without incident.

In

general, the licensee implements effective controls for these

.

evolutions.

However, the inspector questioned the availability of

1

equipment required for gravity flow to the core and expressed concern

that the process for restoring needed equipment may not be sufficiently

controlled.

01.3 Doerator Aid Comouter Installation and Comoensatory Action

a. Insoection Scooe (71707)

l

During the Operator Aid Computer (OAC) installation, the inspector

periodically verified that the Loss of DAC procedure was implemented

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while the OAC was unavailable.

The inspector observed an open main

(

Enclosure 2

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control room door and reviewed the associated compensatory action.

" Control Room Pressure Boundary." dated March 20. 1997, to verify that

the licensee had satisfied selected initial conditions that allowed the

door to remain open.

The inspector also evaluated the licensee's

im)lementation of the compensatory action guidance following receipt of

a Jnit 2 fuel handling building high radiation alarm that occurred on

March 24.

b. Observations and Findinas

During the Unit 2 OAC installation. the OAC was not available for

<

l

automatic surveillance of numerous plant parameters. As a result, the

control room operators were required to implement PT/1/A/4600/09. Loss

of Operator Aid Computer, and perform those surveillances manually'on

specified time intervals. The inspector periodically verified that the

procedure was in use while OAC monitoring was unavailable. Often a

dedicated reactor operator was available to perform this function.

although that could not always be accommodated.

The inspector

determined that the procedure was in place and being implemented when

'

required.

l

The inspector observed that the Unit 2 control room vital access door

was opened on March 22 and was left open continuously to allow passage

'

.

of a flexible ventilation duct (approx. 12 inch diameter). The duct was

.

used to exhaust fumes generated from welding performed to install the

I

replacement operator aid computer in the Unit 2 main control board

panel. The inspector discussed the compensatory actions with

engineering and operations 3ersonnel to determine if the compensatory

actions would ensure that tie control room would pressurize sufficiently

to meet control room habitability requirements during design basis

'

events.

Both operations and engineering personnel stated the design

basis for contrM room pressurization and habitability would be met

provided that initic1 conditions of the compensatory action were

satisfied and that the control room door would be manually closed, after

separating a connection in the duct. if certain plant events (e.g..

safety injection signal) were to occur.

The inspector verified that selected initial conditions were satisfied

and found no discrepancies with the plant conditions that existed at the

time of the inspection.

The inspector observed, however, that the

initial conditions of the compensatory action were not being

periodically verified to ensure that plant changes since the initial

condition verification on March 22 had not invalidated the assumptions

supporting the compensatory action. Operations personnel informed the

inspector that periodic verification of initial conditions for the

compensatory actions was not required.

l

The inspector expressed a concern to the licensee that, because there

l

was a high number of initial conditions required for this particular

compensatory action and because of the relatively long duration of the

Enclosure 2

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replacement operator aid com) uter installation, periodic verification of

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initial conditions may have 3een warranted to ensure that necessary

conditions continued to be met.

Additionally, the licensee recognized

that changes in plant ventilation equipment status created by refueling

outage activities could invalidate the assumptions of the analysis

supporting the compensatory action.

The licensee initiated timely corrective actions to periodically

reverify the initial conditions of the compensatory action.

The

i

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periodicity of the reverification varied based on the potential for the

l

condition to change.

The inspector observed the reverification of the

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initial conditions following implementation of the licensee's corrective

actions.

l

The inspector observed two other minor discreaancies during the review

,

of the compensatory action im)lementation.

T1e control room door was

i

not closed on March 24 when tie Unit 2 spent fuel pool bridge radiation

i

monitor (2 EMF 4) alarmed although this appeared to be a condition for

closing the door.

The inspector determined that the radiological

conditions that caused the alarm were inconsequential and not related to

l

a release (refer to Section 01.5).

The inspector also found that the

accountability log sheet that specified individuals responsible for

manually closing the control room door had not been signed for one day.

.

The inspector determined that the individuals involved were aware of

l

their responsibilities, but had committed an administrative error.

<

The licensee documented the inspector's concerns in Problem

Investigation Process (PIP) Report 0-C97-0988 and initiated actions to

l

determine:

(1) if the response to the alarm was appropriate: (2) the

cause of the administrative error: and (3) if a reverification process

'

for compensatory actions is needed.

I

c. Conclusions

The inspector concluded that control room operators were appropriately

implementing their procedure for Loss of OAC when the OAC was

l

unavailable during the installation process. Additionally, operator

effectiveness in implementing a complex compensatory action was

challenged by numerous initial conditions and the lack of periodic

reverification to ensure that they were being continuously met.

01.4 Boron Dilution Mitiaation System Reliability

a. Insoection Scope (71707)

Du' ring the Unit 2 shutdown for refueling outage 2E0C8. multiple problems

associated with the Boron Dilution Mitigation System (BDMS) were

,

encountered.

The inspector investigated the nature of each problem and

reviewed the work history of the BDMS for both units. The inspector

i

Enclosure 2

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reviewed the FSAR and Technical Specifications (TS) and discussed system

performance and vulnerabilities with engineering personnel.

b. Observations and Findinas

,

The BDMS consists of two trains and is designed to protect the reactor

.

from an inadvertent criticality by automatically stopping the flow of

i

unborated water to the core during shutdown conditions.

Required by TS

in Modes 3, 4. 5. and 6. the BDMS uses two source range detectors to

'

monitor the subcritical multiplication of the reactor core.

An alarm

,

set)oint is continually calculated, and if the setpoint is exceeded,

eitler train of BDMS will automatically shut off both reactor makeup

water pumps, align the suction of the charging pumps to the Refueling

Water Storage Tank (FWST), and isolate flow to the charging pumps from

.

the Volume Control Tank.

Because these functions are automated, no

operator action is required.

Technical Specification 3.9.2 requires both trains of the BDMS to be

operable during Mode 6.

If one or bcth trains are inoperable, the

licensee must either suspend core alterations or verify' that source

+

range neutron flux monitors are operable with alarm setpoints

a)propriately calculated for the current (and, during core reload,

clanging) steady-state count rate.

The licensee also must take

additional actions to verify that audible alarms are available in the

control room and containment, and that reactor makeup water pump flow

rates are within limits.

In addition the BDMS is required operable

during Modes 3, 4 and 5 by TF 3.3.3.11.

kDuringtheUnit2refuelingoutage,multipleproblemswiththeBDMSwere

encountered. On March 25. Unit 2 BDMS interlock testing revealed a

failure to secure the reactor makeup water pumps.

The failure was

attributed to a failed optical isolator.

On March 28 during core

offload to the Spent Fuel Pool, a spike on the B train source range

instrument caused the charging pump suction to swap from the Volume

Control Tank to the FWST.' This spike was attributed to noise generated

by welding activities during the Operator Aid Computer replacement and

exacerbated by a loose plug at the data processing cabinet. A third

problem, which also occurred during the core offload, was associated

with a shutdown monitor that failed to a zero signal reading.

Because

of the latter two problems the BDMS was declared inoperable, and the

required TS actions were performed.

Problems with the BDMS had been encountered periodically in the past.

According to the licensee's Work Management System (WMS), numerous work

requests have been written since 1987 for the BDMS.

Since 1986. 134

work requests have been closed for the Unit 1 BDMS: since 1987. 83 work

requests have been closed for the Unit 2 BDMS. The inspector could not

consistently determine if specific work requesis were generated to

resolve system problems or if they were "onerated for other reasons

(e.g. nameplate installation).

Nonetheles:.. the volume of work requests

Enclosure 2

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related to this system seemed high.

The inspector expressed to the

t

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licensee a concern with BDMS reliability and availability, as well as

the resulting impact (i.e., additional calibrations and monitoring) to

l

control room operators. The licensee had come to the same conclusion

through a system review independent of the NRC's inspection.

Based on

!

their findings, the licensee had recently decided to incorporate the

!

BDMS into the site's Top Equipment Problem Resolution (TEPR) program.

l

c. Conclusions

t

Problems encountered with the BDMS during the' Unit 2 refueling outage

'

. were indicative of historical system performance problems, which affect

plant operation during modes 3. 4. 5 and 6.

The inspector concluded

that, since additional monitoring and calibration activities are

required when the BDMS is inoperable the BDMS has caused additional

~

control room operator workload to compensate for its unreliability. The

licensee has indicated that efforts are being initiated to improve

i-

system reliability and, thereby. reduce operator burden through the TEPR

process.

So that the licensee's efforts to correct this adverse system

.

performance trend can be monitored to resolution, this issue is

'

identified as Inspector Followup Item 50-413.414/97-07-02: Boron

Dilution Mitigation System Reliability Resolution.

.

01.5 Fuel Handlino Buildina Evacuation

a. Insoection Scooe (71707)

'The inspector evaluated the licensee's response to a radiation alarm

resulting in an evacuation of the fuel handling building that occurred

on March 24. The inspector reviewed licensee's procedures, conducted

interviews with involved personnel, and walked down the fuel handling

building.

b. Observations and Findinas

On March-24. the inspector responded to the control room when the

control room operators announced over the public address system the

i

,

evacuation of the fuel handling building.

During this time, the water

'

level in the fuel transfer canal had been lowered to facilitate

maintenance on valve 2KF-122. Fuel Transfer Canal Isolation Valve. The

ins)ector found that the spent' fuel pool bridge radiation detector

(2EiF-4) had alarmed, and annunciator response procedure for alarm 2-

RAD-3 had been implemented. The control room o)erators conservatively

elected.to evacuate the fuel handling building )ecause the ah:r.m was not

expected.- The inspector verified that the control room operators

i

properly followed their procedures and that the appropriate level of

supervisory oversight was maintained during the event.

j

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The inspector also discussed the event with Radiation Protection

'

personnel and found that proper actions were completed.

Radiation

Enclosure 2

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Protection technicians surveyed the area and reported back to the

control room.

Subsequently, the 2FME-4 alarm setpoint was raised to

2

three times the background radiation level in'accordance with approved

!

procedures.

Additionally, the inspector verified that the area survey

map for the fuel handling building was updated, and the associated

i

instrument log for 2 EMF-4 was changed to reflect-the new setpoint.

!

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Because the alarm was not anticipated, the licensee initiated actions to

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evaluate the root cause of the event and determine appropriate

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corrective action.

Discussions with various plant )ersonnel revealed

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that better coordination between affected plant wort groups and a

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possible procedure enhancement were needed during fuel transfer canal

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draining. This would provide for an increase in the alarm setpoint to

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accommodate the expected increase in background radiation levels in the

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area with the canal drained.

!

On March 25. the inspector performed a walkdown of the fuel handling

building for area familiarization.

During the walkdown the inspector

performed a housekeeping assessment with emphasis on the licensee's

'

adherence to foreign material exclusion (FME) requirements. ' The

>

l

inspector found that miscellaneous items (e.g. safety belt, tool bag,

2

face shield. grease gun, and paper) i.ere on the transfer canal catwalk

area and had not been logged into the cleanliness logbook. The licensee

i

.

subsequently issued PIP 2-C97-08/1 to document this NRC observation and

i

address corrective actions.

'

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c. Conclusions

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The inspector concluded that actions by operations and RP personnel .in

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response to the radiation alarm in the fuel handling building were good.

"

!

However, administrative controls over FME were not pro)erly im)1emented

by personnel working near the fel transfer canal in t1e fuel landling

t

building.

01.6 Unit 1 Pressurizer Block Valve Control Circuit Failure

a. Insaection Scone (71707. 61726. 62707)

'

On March 20, Unit 1 pressurizer Power 0)erated Relief Valve (PORV) block

valve INC-33A failed.to. stroke closed w1en the valve control switch was

placed in the closed position during surveillance testing. A similar

failure of this valve had occurred on August 10, 1995. The inspector

reviewed the licensee's immediate actions to comply with TS action

requirements and an associated operability evaluation. The inspector

also reviewed PIP documentation (1-C97-0781 and 1-C95-1204) and the

licensee's evaluation of the potential repeat failure.

'

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Enclosure 2

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b. Observations and Findinos

The block valve is controlled with a three position control switch

(open/close/ override).

During the surveillance test the valve failed to

close when the "close" Josition was selected.

The licensee declared the

-

valve inoperable and suasequently succeeded in closing the valve using

'

the " override" position.

The inspector verified that the licensee met

TS requirements after the valve was declared inoperable (TS 3.4.4.

.

Relief Valves).

Maintenance troubleshooting determined that the failure occurred in an

interlock portion of the block valve's control circuit. The interlock

uses position signals generated from stem mounted limit switches located

,

on the two other Unit 1 pressurizer PORV block valves. An operability

evaluation performed after troubleshooting efforts concluded that the

block valve was operable since it would remain capable of closing as

required using the " override" position.

The licensee's investigation of

.

the previous failure in 1995 found that a limit switch lever shaft had

broken.

The licensee has scheduled work orders to inspect the limit

switches and block valves during the next refueling outage and will

initiate further investigation if the same type of failure has occurred.

J

c. Conclusions

'

.

A Unit 1 pressurizer PORV block valve control circuit failure occurred

.

which is a potential repeat of a previous 1995 failure. The licensee

has planned appropriate actions to determine the cause of the control

'

circuit component failure when the components are accessible at the next

refueling outage.

08

Miscellaneous Operations Issues (92901. 92902)

08.1

(Closed) VIO 50-413.414/94-13-01: Failure To Follow Procedure NSD 703

4

And Station Directive 34.0.5 Requirements.

The inspectors reviewed the corrective actions identified by the

licensee for this violation in letters dated August 15. 1994, and August

8.1995, and verified that these actions were reasonable and complete.

The licensee's evaluation substantiated the violation and identified

'

approximately 600 comaonents which were provided with an identification

'

tag that identified t1e component number, but the tag did not include

the component's noun name as required by the site's procedures. The

inspectors performed a sample inspection of these components and

verified that the identification tag included both the component number

and noun name.

4

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08.2 (Closed) VIO 50-413/95-07-01: Inadequate Modification Procedure

Resulting in Loss of RHR.

TN/1/A/1331/00/01A. Procedure for the Implementation of NSM CN-11331.

Work Unit 01. did not receive adequate cross disciplinary review to

determine operational impact and scheduling to determine a safe plant

condition for implementation. The licensee's response dated April 28,

1995. stated that immediate actions were taken to revise the procedure

and stop work on modification implementation until all modification

packages were reviewed for similar errors. Additionally, the licensee

formed two self-assessment teams to determine root cause of the event.

The modification process was also revised to add new screening criteria

for critical modifications that require an independent Senior Reactor

1

0)erator review to determine safe plant conditions for implementation of

t1ese modifications.

The inspector reviewed corrective action

j

documentation (PIP 1-C95-0203) and verified that the licensee completed

these actions.

08.3 (Closed) VIO 50-413.414/95-07-02: Inadequate Valve Verification

Activities - Two Examples.

l

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Both examples of the violation involved personnel that failed to use

proper verification methods or independent verification of determining

.

l

valve position or valve location.

The licensee's response dated April

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!

28, 1995, stated that procedure revisions and additional training was

l

provided for the plant staff that is involved in these verification

activities.

The ins)ector verified that Operations Management Procedure

2-33. Valve and Breacer Position Verification and Valve Operations, was

revised to provide guidance for verifying the position of deenergized

motor operated valves.

In addition, the licensee provided training to

establish worker skills in error reduction. The inspector concluded

,

that the licensee's corrective actions were appropriate.

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II. Mainwunce

M1

Conduct of Maintenance

1

M1.1 Unit 2 Outaae Maintenance Items

a. Insoection Scope (62707)

l

The resident inspector monitored and inspected various work items during

l

the Unit 2 E0C8 refueling outage.

Among these were: (1) a modification

to replace the 2A and 2B Emergency Diesel Generator (DG) battery

chargers: (2) inspection and preventive maintenance on the 2B DG: (3)

the inspection and reconditioning of valves in the Safety Injection (NI)

system: (4) the repair of Loose Parts Monitoring System Channel 17.

Steam Generator (SG) manway: (5) the inspection of the containment sump

recirculation valve 2NI-185B: and (6) inspection of the A and D Reactor

!

Coolant Pump (RCP) number 1 seals.

The inspector discussed the

Enclosure 2

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maintenance activities with the licensee, obtained copies of the work

packages and observed portions of the maintenance in progress.

b, Observations and Findings

l'

(1)

The Unit 2 125 Volt DC DG battery chargers were replaced under

station modification CN-21360.

The inspector reviewed the work

Jackages associated with TN/2/A/1360/00/02E, which governed the A

Xi battery charger replacement., and TN/2/A/1360/00/03E, which

governed the B DG battery charger replacement. The inspector

verified that an 8-hour load test on DG chargers- 2A and 28 a

polarity check, output voltage check and current check were

,

successfully completed before the battery chargers were installed.

Steel frames and grout pads were fabricated for the chargers. The

inspector also verified that provisions for maintaining electrical

i

separation, fabricating and installing electrical enclosures,

grounding cables, sealing the cable terminations, and using

crimping tools were included in the work packages.

Cable

installation was ')rocedurally controlled, and electrical

isolations and ca]le terminations were recorded in the associated

procedure. A charger capacity test was satisfactorily performed,

the battery was equalized and charged, batteries were inspected.

.

and the charger's high and low voltage relay alarms were

calibrated.

(2)

The inspection and maintenance plan for the 2B DG included

activities typically performed on a five-year interval. The

l

inspector observed portions of the activities in progress and

reviewed the work package and associated work orders,

The

licensee disassembled sections of the DG: cleaned the engine

block; replaced hoses: refurbished the engine-driven fuel oil

pump: inspected cams and rollers: inspected the jacket cooling

water pump drive gear: inspected strainers for the starting air

system; and inspected and refurbished a temperature regulating

valve in the DG jacket cooling water system.

(3)

Multiple check valves, suspected of leaking, were inspected during

l

the outage. The licensee inspected valve 2NI-171, Safety

Injection pumps to RCS loop C cold leg injection header check

,

valve, and determined that the valve had low seating contact.

A

l

minor modification was generated, and the disc was replaced with a

new disc of a different design that provided better seating

integrity.

Valve 2NI-175. RHR header A to RCS Loop C cold leg check valve,

was inspected: the valve was cycled, and the disc operated freely

,

without binding. The valve body and disc seats had no indication

H

of degradation.

The valve body and disc seats were cleaned, and a

'

visual inspection revealed wide seat contact.

Enclosure 2

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Valve 2NI-176 RHR Header A to RCS Looi D cold leg check valve.

'

showed no evidence of seat wear or leacage. The licensee cleaned

the seating surfaces and determined that they were finely. polished

.'

with no indication of degradation.

l

The disc in valve 2N!.-169. Safety Injection pumps to RCS lcop D

cold leg injection header, was replaced, and the valve body seat

l

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was lapped until good contact could be visually verified. A-small

!

defect was polished out of the valve bonnet.

The defect was

i

believed to have caused minor external leakage in December 1995

and had been seal welded at that time to stop the leakage.

The inspector did not identify any concerns associated with the NI

system check valve maintenance.

(4)

Unit 2 Loose Parts Monitoring System Channel 17. SG manway, was

repaired during a forced outage in December 1996. The channel had

been declared inoperable on January 2, 1996.

Subsequent

troubleshooting revealed that the failure of the channel

originated in the field. The licensee initiated a work request to

,

'

repair the channel during an outage window, at which time the

necessary containment entry could be made. To notify the NRC that

Channel 17 of the Loose Parts Monitoring System was inoperable for

.

.

longer that 30 days, the licensee submitted a s)ecial report on

l

February 11, 1996, in accordance with Selected .icensee

Commitment Section 16.7-4, and TS 6.9.2.

The inspector discussed the repair with licensee personnel,

reviewed the associated work order. WO 96000758-01, and verified

,

that the channel )roblem had been corrected. The licensee had

determined that tie acoustic sensor' had an open _ connector at the-

female hard line connector point. The sensor was replaced and-

!

satisfactorily tested. The channel was returned to service on

December 16, 1997.

(5)

Prior to the last refueling outage-(2EOC7) the licensee determined

!

that containment sump recirculation valves NI-184A and NI-185B.

l

double-disc gate valves, were susceptible to pressure locking.

!

During 2EOC7 the licensee im)lemented a station modification to

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install a bonnet vent on eac1 sump recirculation valve.

The

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1

bonnet vents provided a relief path from the valve body to the

residual heat removal (RHR) aump discharge line to preclude

pressurization in the valve Jody and subsequent wedging of the

i

valve discs into their respective seats. The bonnet vent valves

'

were intended to remain open during full )ower o)erations,

although they could be. closed to isolate RHR leacage past the

containment-side valve disc.

7

I

During startup from the- previous refueling outage. 2EOC7.- the

i

licensee determined that the containment-side seat of 2NI-185A was

Enclosure 2

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leaking.

Since the bonnet vent valve (2NI-488) bypassed the RHR

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suction-side disc a minor flow 3ath was created from the FWST.

L

via the RHR suction header. to t1e containment sump.

To block the

!

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leakage, vent valve 2NI-488 was locked closed. A work order was

i

generated to inspect and repair 2NI-185B during 2E0C8.

l

The licensee opened the valve to inspect the seatirig surfaces

l

l

during the refueling outage: the inspection results were

~

documented in PIP 2-C97-1066. At several locations around the

perimeter of the containment-side valve body seat, small

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semicircular indicat ons were visible. The containment-side disc

i

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seat had similar marks where the two surfaces had mated. The

i

licensee could not determine why the pattern was present on the

'

l

valve body seat, nor coula the valve vendor explain these

!

indications. The indications in the seat surfaces were the likely

!

!

cause of the seat leakage during the previous operating cycle.

)

l

The licensee opted to leave the valve in its as found condition to

!

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avoid disturbing the seating of the RHR-side disc. The inspector

i

questioned this decision, since they had been aware of the seat

,

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leakage during the preceding operating cycle and had ample time to

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plan for re) air during the refueling outage.

The licensee

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explained tlat extensive time and resources could be allocated to

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improve the containment-side di.;c seating, but that improvement

j.

could not be guaranteed and that the RHR-side disc seating

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integrity could be disturbed in the process.

i

To test valve seating integrity.of the containment-side disc. the

<

licensee applied 50 psig from the RHR pump side of the valve with

l

vent valve 2NI-488 closed: no signs of leakage into the

,

'

containment sump were identified.

Valve 2NI-488 was then' opened.

!

!

and leakage into the sump was observed.

Valve DI-488 was then

closed, and leakage into the sump was isolated oy the seating

l

integrity of the RHR-side disc and the bonnet vent valve. An

i

operability evaluation, documented in PIP 2-C97-1172. stated that

(1) valve 2NI-488 will be administratively controlled in the-

closed position, and (2) valve 2NI-185A is operable with 2NI-488

closed.

The inspector concluded that the o)erability evaluation

,

i

and actions taken to address seat leakage w1ile accounting for

!

pressure locking and thermal binding were appropriate.

(6)

The inspector observed RCP seal inspections and maintenance. The

!

ins)ector also reviewed the task completian comments associated

wit 1 work orders 96098973-01 and 96098974-01 (for 2A and 2D RCP

seal work, respectively). The 2D RCP numoer 1 seal was cleaned

and inspected verified to be in good condition. and reinstalled.

A chip was found in the outer edge of the 2A 'RCP number 1 seal

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surface. A new set of stationary and running seals was installed,

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and the maintenance personnel verified that the seal moved freely

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up and down.

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The inspector noted that RCP seal work was conducted in confined

areas around the RCPs.

The work areas were difficult to access

and cramped.

In addition, cleanliness and lighting levels during

the maintenance activities were adversely affected by the cramped

working spaces.

c. Conclusions

The inspector concluded that, in general, outage-related maintenance

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activities were ap]ropriately conducted.

Although multiple barriers to

minimizing the risc of human error during RCP seal maintenance were

noted, the ins)ector was unaware of any human performance problems

associated wit 1 the work.

M1.2 Unit 2 Nuclear Service Water Pumo Motor Reolacement

a. Insoection Scope (62707)

The inspector reviewed the licensee's resolution to elevated vibration

levels associated with the 2B nuclear service water pump / motor assembly.

The 2B nuclear service water pump has experienced intermittent periods

of elevated vibration since 1994.

During the inspection period, the

licensee identified problems with the condition of the s

service water replacement motor stored in the warehouse. pare nuclear

.

Accordingly,

the inspector reviewed the results of previous licensee assessments of

spare motor storage practices, previous motor failures, and an ongoing

licensee assessment of maintenance and storage practices for spare

motors.

b. Observations and Findinas

The 28 Nuclear Service Water pump is a smooth running pump with normally

low measured vibration levels.

In 1994 and 1995 the pump / motor assembly

3eriodically experienced an increase in vibration relative to its past

)aseline performance and also relative to the other nuclear service

water pumps. The relative increase in vibration levels caused the pump

to enter Alert levels although it continued to remain in the smooth

running range,

As a result of this experience, the licensee performed

extensive inspection of this pump and motor during the current refueling

outage.

Internal inspection of the pump showed no damage or

degradation.

Vibration measurements made during an uncoupled run of the

motor indicated that the source of elevated vibrations was confined to

the motor. Based on additional analysis of vibration dr.ta performed by

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Electrical System Support (ESS) personnel, the licensee determined that

an internal rub was occurring in the motor and elected to replace it.

The spare nuclear service water pump motor developed severe oil leaks

from its lower bearing during initial check out runs performed in the

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motor test shop prior to its installation.

Inspections of the saare

motor internals performed by an offsite vendor determined that tie lower

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bearing surfaces were partially melted due to rubbing or inadequate

lubrication.

Additional testing revealed more problems and the spare

motor was considered unacceptable for use and required extensive rework

and repair.

The licensee subsequently performed internal inspections of

the installed nuclear service water pump motor and determined the cause

of the eleyated vibration resulted from mechanical looseness in the

,

upper bearing components. An off center condition in the lower bearing

housing was also discovered.

The licensee corrected these

adeficiencies, which eliminated the elevated vibration characteristic as

measured in uncoupled runs and coupled inservice pump tests.

In 1996, a residual heat removal pump motor failed soon after functional

testing. The licensee determined that poor storage conditions may have

contributed to this failure (refer to NRC Inspection Report 96-13). The

licensee has recently performed two assessments of motor storage and

handling practices and identified several findings and recommendations.

Inspector Followup Item (IFI) 50-413.414/97-07-03, Review Corrective

Actions For Storage and Handling Assessment Findings, is identified to

verify that the licensee has completed corrective actions resulting from

the followirig assessments:

(1) Assessment Report CTS-09-96. Electric

Motor P.M. - 12/2/96; and (2) Assessment Report SA-97-61(CN)(SRG),

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Assessment of Warehouse Material Condition - 4/23-28/97.

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c. Conclusions

The licensee's resolution of long-standing elevated vibration levels

,

associated with the Unit 2B nuclear service water pump motor was very

good.

Deficiencies identified with a spare nuclear service water pump

motor, a previous motor failure, and findings identified by licensee

assessment of warehouse storage and handling 3ractices raised questions

about control and storage of spare motors. T1e issue is identified as

an Inspector Followup Item and will be reviewed during a future

inspection.

M2

Maintenance and Material Condition of Facilities and Equipment

M2.1 Observation of Unit 2 Inservice Insoection Work Activities

a. Insoection Scope (73753)

The present Unit 2 E0C8 refueling outage was the first outage, of the

first inspection period, of the second inservice inspection interval.

The applicable code for Unit 2, for the second inservice inspection

interval was the American Society of Mechanical Engineers (ASME) Code

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Section XI, 1989 Edition, no Addenda. The inspector reviewed

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documentation and observed ultrasonic, magnetic ) article, and liquid

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penetrant examination activities to determined w1 ether the inservice

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inspection (ISI) activities were performed in accordance with Technical

specifications (TS), the applicable ASME Code, and/or requirements

imposed by NRC/ industry initiatives.

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b. Observations and Findinos

The inspector reviewed the ISI outage examination plan and certification

records for all NDE examiners aerforming ISI examinations this outage.

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The following procedures, whic1 were used in the examination activities

observed by the inspector, were reviewed for technical content:

NDE-600. " Ultrasonic Examination of Similar Metal Welds in Wrought

Ferritic and Austenitic Piping." Revision 9

NDE-610. " Ultrasonic Examination of Dissimilar Metal Welds and

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Cast Austenitic Welds Using Refracted Longitudinal and Shear

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Waves." Revision 4

NDE-660 " Ultrasonic Examination of Reactor Pressure Vessel Head

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to Flange Welds." Revision 2

NDE-25. " Magnetic Particle Examination." Revision 17

.

NDE-35. " Liquid Penetrant Examination." Revision 16

.

Examinations of the following components were also observed by the

inspector to determine if the examination procedures were followed,

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whether examination personnel were knowledgeable of the examination

method and operation of the test equipment, and if the examination

results and evaluation of the results were recorded as specified in the

ISI program and NDE procedures.

. Welds Examined

NDE Method Used

2RPV-101-101***

Ultrasonic Examination

2RPV-102-101***

Ultrasonic Examination

2CA-59-8

Ultrasonic Examination

2CA-59-11

Ultrasonic Examination

2RPV-101-101

Magnetic Particle Examination

2CA-59-8

Magnetic Particle Examination

2CA-59-11

Magnetic Particle Examination

2NV-242-3

Liquid Penetrant Examination

2NV-242-4

Liquid Penetrant Examination

2NV-242-10

Liquid Penetrant Examination

2NV-242-11

Liquid Penetrant Examination

2RPV-W80-101SE

Liquid Penetrant Examination

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2RPV-W81-101SE

Liquid Penetrant Examination

2RPV-W82-101SE

Liquid Penetrant Examination

2RPV-W79-101SE

Liquid Penetrant Examination

2RPV-W80-101

Liquid Penetrant Examination

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2RPV-W81-101

Liquid Penetrant Examination

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2RPV-W82-101

Liquid Penetrant Examination

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2RPV-W79-101

Liquid Penetrant Examination

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        • Note: Only portions of the 0 degree and 45 degree scans for these

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reactor vessel head welds were observed due to radiation dose

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limitations.

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c. Conclusion

NDE personnel certifications records, weld examinations, and NDE

examination procedures were in accordance with Code requirements.

M2.2 Observation of Unit 2 Steam Generator Eddy Current Data Acouisition

Activities

a. Insoection Scooe (73753)

The inspector reviewed documentation and observed eddy current data

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acquisition activities to dstermine whether these activities were

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performed in accordance with Technical Specifications (TS), the 1989

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Edition of Section XI to the ASME Code, and requirements imposed by

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NRC/ industry initiatives.

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b. Observations and Findinas

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The licensee was performing bobbin coil eddy current examinations of 62%

of the tubes in all four steam generators for Unit 2.

In addition, a

25% sample of the hot leg tube sheet transitions in each steam generator

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will be examined using a motor rotating pancake coil (MRPC). At the

time of this ins)ection the licensee had just started the examination

activities and t1e data acquired was being sent directly to the McGuire

Nuclear Plant for analysis.

Therefore, the inspector's examination of

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these activities was limited to review of the outage eddy current

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inspection plan, examiner and equipment certifications, and review of

examination procedures No. NDE-707 Revision 3, "Multifrequency Eddy

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Current Examination of Non-Ferrous Tubing. Sleeves and Plugs Using a

Motorized Rotating Coil Probe", and No. NDE-701 Revision 3.

"Multifrequency Eddy Current Examination of Steam Generator Tubing at

McGuire. Catawba and Oconee Nuclear Stations and observation of the eddy

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current data acquisition process,

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c. Conclusion

Review of the eddy current outage plan, equipment setup and acquisition

procedures, personnel and equipment certifications, and observation of

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data acquisition activities revealed that required documentation was

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available and complete. and data acquisition personnel were

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knowledgeable of the eddy current examination process.

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M2.3 Unit 2 Flow Accelerated Corrosion (FAC) Proaram

a. Insoection Scooe (49001)

The inspector held discussions with the licensee's erosion / corrosion

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engineers to determine the scope of FAC examinations scheduled for this

outage: the condition of the plant piping as revealed by inspection: the

extent of pipe replacement recuired: and whether proper examination

expansion was performed when cefective components were found.

b. Observations and Findinas

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The licensee's FAC program for Unit 2 was based on the Electric Power

Research Institute's (EPRI) Document No. NSAC-202L. " Recommendation for

an Effective Flow Accelerated Corrosion Program." Revision 1.

In

addition. EPRI's CHEC Works Computer Codes were used, as well as

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portions of the licensee's prev'ous program for erosion / corrosion to

identify components which will require examination.

Initially, a sample

of 55 components were scheduled for ultrasonic examination during the

EOC-8 refueling outage.

The sample also included the entire component.

upstream and downstream of the initial component. The licensee planned

to replace six components without further examination, based on

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corrosion growth rates confirmed last outage.

The examination of

.

components for FAC this outage were approximately 40% complete when

audited by the inspector. As a result of these examinations, five

additional components will be replaced this outage.

The inspector

verified that expansion ins)ections.were correctly performed as a result

of the components found to 3e unacceptable based on inspections

performed this outage.

The inspector also inquired as to why the

initial inspection sample was so small.

The licensee stated that

smaller samples with a high volume of essential components. based on

tracking and trending was now possible on Unit 2 for the following

reasons:

Significant previous replacements of components with

.

erosion / corrosion resistant materials.

Changes in secondary chemistry control have reduced wear rates

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significantly.

The entire upstream and downstream components from a sample

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selected for inspection are also examined.

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Unit 2 was designed with heater drains and moisturizer separator

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reheater drains which have erosion / corrosion resistant materials

downstream of all control valves.

FAC program maturity.

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The inspector agreed with the licensee's reasoning.

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c. Conclusion

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The licensee has implemented an effective program for the detection of

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flow accelerated corrosion in components.

This program was based on

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recommendations found in recognized industry standards.

M7

Quality Assurance In Maintenance Activities

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M7.1 Maintenance Self Assessment Prooram

a. Insoection Scone (62707. 40500)

The inspector reviewed the status of maintenance and work control self-

assessment programs.

The inspection included review of NSD 607. Self-

Assessments; maintenance and work control annual assessment plans for

1996 and 1997: selected self-assessment reports; and maintenance / work

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control performance indicators,

b

Observations and Findinas

The licensee's self-assessment program consisted of two types of self-

assessments, routine and non-routine.

Routine assessments were

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performed on a quarterly or semi-annual basis and included topics such

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as PIPS, Job Observations. Rework. Material Condition / Housekeeping. Work

Order Quality. Budget. Radiation Dose / Contamination. Planning, and Work

Control Process.

Non-routine assessments were performed when the need

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was apparent to management to assess a certain area or function. Some

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examples were Procedure Use and Adherence. Environmental Compliance.

Pre-job Briefings. Control of Vendors, and Work Task Skills.

Corrective

actions from the self-assessments were tracked for completion through

PIPS.

The inspector noted that the self-assessments that were reviewed

effectively identified areas for improvement, and appropriate corrective

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actions were recommended and entered in the Problem Investigation

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Process for resolution.

Of the routine assessments reviewed the

inspector considered the quarterly assessment of Job Observation Trends,

initiated in 1997, to be an effective use of the data generated by first

line supervisor observations.

Since the initiation of the Maintenance / Work Control Self-Assessment

Programs in mid and late 1995. performance indicators such as work order

backlog, schedule efficiency, and control board indication problems all

showed improving trends.

c.

Conclusion

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Based on the inspection described above. the inspector concluded that

the maintenance / work control self-assessment programs effectively

identified areas for improvement and appropriate corrective actions.

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The self-assessments apparently contributed to improvemert. in the

performance of the Maintenance and Work Control organizations.

III. Enaineering

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Conduct of Engineering

El.1 Unit 2 Control Rod Tio Crackina

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a. Insoection Scoce (61726. 37551)

During routine outage related examinations of Unit 2 control rod .

assemblies, the licensee identified a higher than expected number of

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control rods with tip cracking. The inspector reviewed the licensee's

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testing procedure, results of the examinations, and corrective actions

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for test failures,

b. Observations and Findinos

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Industry experience has shown that control rods develop tip cracking as

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a result of cladding interaction caused by swelling of the absorber

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material inside this portion of the rods. . Tip cracking and other

potential control rod defects such as mechanical wearing are monitored

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every refueling outage by the licensee using procedure PT/0/A/4150/26.

Rod Control Cluster Assembly (RCCA) Ultrasonic / Eddy Current Testing.

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The inspector. discussed the results of the testing with reactor

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engineering personnel.

The inspector observed that twenty.six control

rod assemblies were found with indications of tip cracking.

This

exceeded the expected number of twelve control rod assemblies aredicted

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to have tip cracks

The licensee ordered additional rod assem) lies

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fabricated by the vendor and replaced each control rod assembly that had-

evidence of tip cracking.

The inspector verified by reviewing control

rod assembly deficiency evaluations that the twenty six assemblies were

replaced.

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c. Conclusions

The licensee's actions to replace all control rod assemblies that had

evidence of tip cracking were appropriate.

E2

Engineering Support of Facilities and Equipment

E2.1 Review of Tentative Repair Activities for the Manway Cover on the Unit 2

Pressurizer

a. Insoection Scone (62001)

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The Catawba Unit 2 pressurizer manway cover experienced a leak during

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the end of cycle 8 shutdown for refueling.

To repair the leak, the

licensee elected to use an alternate method of repair consisting of a

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welded diaphragm, in lieu of a flexitallic gasket.

The licensee also

planned to replace the bolts and nuts on the manway cover with studs and

nuts.

Another issue addressed in this modification was the inspection

and clean-up of the boric acid which had leaked from the flange of the

manway behind the insulation on the pressurizer.

The inspector

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reviewed this modification to ensure that documentation required for

this repair was available, and that inspection and cleanup of the boric

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acid crystals behind the pressurizer was properly addressed.

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b. Observations and Findinas

In 1987, the licensee experienced several stuck bolts on the Unit 1

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pressurizer manway. At that time the licensee used the alternate method

of repair delineated in the Westinghouse Technical Manual for the

pressurizer.

This repair consisted of using a welded diaphragm, in lieu

of a flexitallic gasket.

In addition, the licensee substituted studs

for the bolts used in the manway flange. At that time the licensee also

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realized that this same modification may some day be required for Unit

2. so 10 CFR 50.59 evaluations for the alternate modification method and

calculations for the stress analysis of the studs and nuts were

conducted for each Unit in 1987.

The inspector reviewed this

documentation as well as the Westinghouse Pressurizer Technical Manual

and drawings for this alternate method of repair. The information

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reviewed was found to be satisfactory.

The inspector was initially concerned with the licensee's tentative

plans to remove insulation only from the top and bottom of the

pressurizer in order to flush the boric acid crystals from behind the

insulation, and to use technical justification based on boric acid

corrosion rates documented in an EPRI document (TR-102748S) for

acceptance of any possible damage to the pressurizer.

The inspector's

concern was based on the fact that the corrosion rates given in the EPRI

document differed significantly from the corrosion rates established by

Westinghouse under similar conditions and documented in NRC Generic Letter 88-05 " Boric Acid Corrosion of Carbon Steel Reactor Pressure

Boundary Components in Pressurized Water Reactor Plants".

In addition,

the inspector did not believe that the plan to use technical

justification met the intent of Catawba's Nuclear Site Directive 3.3.16.

which stated. "When there is evidence that boric acid has run under

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insulation remove enough insulation during the inspection 3rocess to

assure all boric acid has been identified and evaluated. S1ould the

investigation reveal no damage to the contaminated components, the area

is to be cleaned until free of visible borori crystals." During

discussions held with senior licensee management, the inspector was

informed that the plans for boric acid damage examination and flushing

on the pressurizer which were identified to the inspector were very

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' tentative and only one of many options being considered. The inspector

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was also informed that a meeting on this issue was planned for following

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week and the decisions reached in this meeting would be forwarded to the

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inspector for review.

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On April 9.1997, the inspector was informed of the licensee plans for

inspection and cleaning of boric acid on the pressurizer.

These plans

would remove three additional sections of insulation and would allow

visual inspection to be performed in spot locations from the top to the

bottom of the pressurizer. The only disadvantage was visual inspection

could only be performed on the lower side of each of the sup) ort rings

except the top support ring. The licensee proposed that teclnical

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justification be used for the acceptance of the up)er portion of each

support ring using the EPRI criteria which Westinglouse agreed was

a)propriate for this corrosion wear application.

These actions resolved

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t1e inspector's concerns.

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The licensee )lanned to flush the pressurizer shell with hot water for

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four to five lours in an attempt to dissolve the crystals and remove

them from the carbon steel surface. To verify that the flushing process

was effective in removing the boron, the licensee planned to collect

water samples hourly at the base of the pressurizer and obtain data on

boron concentrations, expecting the concentrations to decrease over

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time. The inspector questioned the confidence level of the validation

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plan as a function of sampling frequency, and asked if an hourly sample

would provide sufficient data to verify that boron concentrations were

indeed decreasing over time. The licensee agreed that more frequent

.

sampling would yield a more robust conclusion and planned to sample the

flushing water every half hour. The ins)ector reviewed the results of

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the pressurizer flushing, documented in )IP 2-C97-0952. and concluded

that the flushing plan was effective in removing any dried boric acid

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from the pressurizer shell.

c. Conclusions

The inspector concluded that documentation for the modification of the

Unit 2 pressurizer manway was satisfactory and engineering

considerations for modification, inspection, and cleaning of the

pressurizer shell were very good.

Results of the boric acid cleanup

indicated that the plan had been effective.

E2.2 Desian Control

a. Ir;soection Scope (37550)

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The inspector reviewed modifications being implemented during the Unit 2

outage.

A)plicable regulatory requirements included Regulatory Guide 1.64 and AiSI N45.2.11-1974. Quality Assurance Requirements for the

Design of Nuclear Power Plants 10 CFR 50.59,10 CFR 50 Appendix B the

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licensee's Quality Assurance Topica'l Report (Duke-1-A), and associated

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design control implementing procedures.

The following modifications

were reviewed:

VN 8303H

Replacement of Limitorque Motors on 2NI-54A. 2NI-65B.

.

2NI-76A. and 2NI-183B

CN 21377

Modify Safety Injection (SI) Logic to Delete Low Stear

.

Pressure Input

CN 21375

Upgrade Allowable Temperature for Some Auxiliary Feed

.

Water (CA) Piping.

b. Observations and Findinas

The specified post modification testing requirements on the above

modifications adequately verified the design function of the modified

equipment.

Implementation of the SI signal deletion (CN 21377) resulted

in damage to six process cards in the Solid State Protection System

cabinet due to short circuits experienced during wiring terminations.

The damaged cards were identified during post modification testing.

Appropriate actions were initiated to replace the damaged cards and

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verify the integrity of the remaining installed cards.

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Replacement Motor Operated Valve Limitorcue motors (VN 8303H) were set

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up using the VOTES testing procedures anc implementing the applicable GL 89-10 requirements.

The modification was required because tie original

size motors for the NI valves were not available.

Cracks were found on

the motor shafts' key way of the installed motors.

Post modification

verification was accomplished by Quality Control inspections for the CA

piping support modifications to upgrade the allowable piping temperature

(CN 21375).

The 50.59 evaluations for the modifications were adequate. A regulatory

issue was pending on the 50.59 evaluation for the CA piping upgrade (NRC

Inspection Report 50-413.414/96-03).

The SI logic signal deletion

safety evaluation was documented in licensing amendments 158 and 150.

c. Conclusion

Regulatory design control requirements were appropriately implemented

for the Unit 2 outage modifications reviewed during this inspection.

E4

Engineering Staff Knowledge and Performance

E4.1 Identification and Correction of Eauioment Problems

a. Insoection Stone (37550)

The inspector reviewed the licensee's actions related to the

identification and resolution of MOV limitorque motor shaft cracking.

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Applicable regulatory requirements included 10 CFR 50 Appendix B and the

licensee's Topical Quality Assurance Program.

b. Observations and Findinas

industry experience reports in 1995 and late 1996 noted examples of

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motor shaft key way cracking in large high speed limitorque MOV motors.

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The reports generally indicated the problem occurred in 3600 rpm motors

sized at 80 ft-lbs and larger. There were ten applications identified

,

at Catawba which included the four cold leg accumulator isolation valves

)

and the NI-183 valves on each unit. The licensee implemented a motor

shaft inspection into the GL 89-10 program in 1996.

No cracks were

identified on the Unit 1 valves inspected during the previous outage.

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There were cracks identified on three Unit 2 valves inspected during the

current outage.

Replacement motors of the original sizes were

unavailable therefore a minor modification was implemented to change

the motor sizes.

The original 175 ft-lb motor on 2NI-183B was replaced

with a 150 ft-lb motor from Cold Leg Accumulator valve 2NI-54.

The

original 150 ft-lb motors on 2NI-54A. 2NI-65B and 2NI-76A were replaced

with 80 ft-lb. 80 ft-lb. and 100 ft-lb motors, respectively.

Valve

motor torque switch settings and parameters were revised to meet the

recuirements of the GL 89-10 program and motor / valve application.

Adcitionally, the associated motor control center overload heaters were

.

replaced on each valve to be consistent with the motor protection

requirements.

c. Conclusion

4

The identification and correction of MOV shaft key way cracking in Unit

2 safety injection system valves was a good example of engineering

identification and resolution of equipment problems.

Industry operating

experience was appropriately incorporated into licensee activities and

effectively eliminated a potential safety-related equipment failure

'

mechanism.

E8

Hiscellaneous Engineering Issues (92903)

E8.1 .(flosed) VIO 50-413.414/96-13-04: Inadequate Design Controls - Two

Examples

Example 1-Selection of Main Steam Isolation Valve (MSIV) Solenoid

Valves:

This item identified a discrepancy where the nameplate design

rating of MSIV solenoid valves was less than the maximum design pressure

of the instrument air system. The ins)ector reviewed the licensee's

response dated November 6. 1996.

The Jnit 1 solenoid valves were

replaced with aapropriate valves prior to identification of the

discrepancy.

T1e valve manufacturer certified by letter that the

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existing Unit 2 solenoid valves were acceptable until replacement at the

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next refueling outage. The inspector verified that the Unit 2 solenoid

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valves were replaced with upgraded valves during this refueling outage

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(MW0s 96070278. 96070289. 96070280. 96070287) and testing of the

replacement solenoid valves was performed satisfactorily (PT

2/A/4200/09. Engineered Safety Feature Actuation Periodic Test).

Examole 2-Standby Shutdown System (SSS) Make-uo Pumn . Calculation - This

item identified calculation design input errors '

'd to the system

conditions and pulsation damper which were useo

.wify the Net

4

Positive Suction Head (NPSH) for the SSS make-up pum). The licensee's

November 6. 1996, response to the violation stated tie design inputs for

the SSS make-up pum) sizing calculation and the damper design would be

evaluated and opera]ility for the Unit 1 and 2 pumps verified. The

inspector reviewed the licensee's completed corrective actions and

verified that the in)ut errors were resolved. Additionally, the actions

to assure pump opera]ility were completed.

E8.2 (Closed) DEV 50-413.414/92-01-03.: Breaker Coordination

This deviation was closed based on NRC Inspection Report 50-413.414/96-

19.

E8.3 (Closed) VIO 50-413.414/96-12-03: Inadequate Design Controls For

Ensuring Containment Crane Wall And Floor Drain Screens Implemented

Design Requirements.

.

This item identified containment crane wall penetrations and floor drain

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screens that did not implement design requirements developed to preclude

transport of debris to the Emergency Core Cooling System sum) screens.

The licensee's October 29, 1996. violation response stated tlat the

crane wall Jenetrations were filled with cualified foam to preclude any

flow throug1 them and modifications were ceveloped correct the screen

size of the floor drain screens.

The inspector reviewed the licensee's

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completed corrective actions, including minor modifications (CNCE-8116.

)

8139. 8186) and drawing revisions (CN-1070-5. rev. 14).

The inspector

also performed a walkdown of the unit 2 containment building and

verified that the modifications were installed.

IV. Plant Support

R1

Radiological Protection and Chemistry Controls

R1.1 Tour of Ridioloaical Protected Areas

a. Insoection Scooe (83750. 71750)

The inspectors reviewed implementation of selected elements of the

licensee's radiation protection program as required by 10 Code of

Federal Regulations (CFR) Parts 20.1201. 1208, 1501. 1502. 1601, 1703.

i

1802. 1902, and 1904.

The review included observation of radiological

protection activities, including personnel monitoring controls, control

Enclosure 2

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of ra'dioactive material, radiological postings, and radiation area /high

radiation area controls,

b. Observations and Findinas

During tours of the Auxiliary Building and radioactive waste

!

storage /handhng facilities. the inspector reviewed survey data and

'

performed selected independent radiation and contamination surveys of

radioactive material storage areas.

Observations and survey results

determined-the licensee was effectively controlling and storing

radioactive material.

'

i

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~The inspector reviewed records for selected employees who had recently

.

!

worn respiratory protection equipment. The inspector verified that for -

<

the records reviewed, each worker had successfully completed respiratory

l

protection training, was medically qualified, and was fit-tested for the

l

specific respirator type used in accordance with licensee procedural

!

requirements. All respiratory protection equipment observed during

facility tours was being maintained in a satisfactory condition.

The

-

licensee had continued to implement engineering controls for respirator

reductions.

During plant tours, the inspector observed that Extra High Radiation

.

,

Areas were locked as required by licensee procedures. The inspector

l

also observed dosimetry controls for these areas were also established

in Radiation Work Permits (RWPs) as required by licensee procedures.

E

t

The licensee's records indicated that the licensee was maintaining

2

approximately 145,000 square feet (ft ) of floor space as a

P

Radiologically Controlled Area (RCA).

Records also showed that the

licensee maintained approximately 800-1000 ft2 (or less than 1 percent)

of the RCA as contaminated area during non-outage periods.

During the-

current outage period, the licensee was maintaining approximately 1200

'

2

.

ft as contaminated area.

The inspectors reviewed Personnel Contamination Event (PCE) reports

t

prepared by the licensee to track, trend, determine root cause, and any

necessary followup action. Approximately 49 PCEs had occurred in 1997:

of which, approximately 38 PCEs had occurred during the current Unit 2

outage.

The inspectors reviewed PCE log sheets for the past three years

and noted PCEs continued to trend downward. The licensee attributed

this reduction to several planned contamination control initiatives,

.uch as: increased followup with workers following contamination events:

,

reduction of contaminated areas: and reductions in radioactive waste.

!

During facility tours. the inspectors observed that survey

instrumentation and continuous air monitors observed in use within the

-

!

RCA were operable and currently calibrated. The inspectors observed a

survey instrument (portable frisker) in the Unit 2 Reactor Containment

(

Building which had not been source checked as required by licensee

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Procedure HP/0/B1003/22. Paragraph 4.9.

The licensee conducted an

-

immediate investigation and located another frisker in the Unit 2

Reactor Containment Building which was available for use in the area

that had not been source checked.

The licensee removed both instruments

from the work area and performed a source check of the instruments to

verify operability.

Both instruments source checked satisfactorily.

The licensee also initiated a Problem Investigation Process (PIP) report

to investigate the problem. The inspectors informed the licensee that

using survey instruments that had not been source checked was a

violation of licensee procedure and TS 6.8.1. Procedures and Programs.

However, based on the licensee's immediate corrective actions and the

safety significance of the circumstances. this licensee identified and

corrected violation is being treated as a Non-Cited Violation consistent

,

with Section VII.B.1 of the NRC Enforcement Policy.

NCV 50-413.414/97-

07-04:

Failure to Source Check Survey Instruments as Required by

Licensee Procedures.

The ins)ectors reviewed controls for entering the RCA and performing

work. T1ese controls included the use of RWPs to be reviewed and

understood by workers prior to entering the RCA.

The inspectors

reviewed selected RWPs for adequacy of the radiation protection

requirements based on work scope, location, and conditions.

For the

RWPs reviewed, the inspectors noted that appropriate protective

.

clothing and dosimetry were required.

During tours of the plant, the

inspectors observed the adherence of plant workers to the RWP

requirements.

The inspectors also verified the licensee was effectively

managing controls for any declared pregnant women in regards to

,.

embryo / fetus doses as required by 10 CFR 20.1208. The licensee was

holding current personnel dosimetry accreditation from the National

,

Voluntary Laboratory Accreditation Program (NVLAP) as required by 10 CFR 20.1501.

c. Conclusions

Based on observations and procedural reviews, the inspectors determined

the licensee was effectively maintaining controls for personnel

monitoring. respiratory protection, control of radioactive material,

radiological postings, and radiation area /high radiation area controls

as required by 10 CFR Part 20.

One NCV was identified for failure to

source check survey instruments as required by licensee procedure.

R1.2 Occuoational Radiation Exoosure Control Proaram

l

a. Insoection Scooe (83750)

The inspectors reviewed the licensee's implementation of 10 CFR

'

20.1101(b) which requires that the licensee shall use, to the extent

practicable, procedures and engineering controls based upon sound

radiation protection principles to achieve occupational doses and doses

,

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to members of the public that are As Low As Reasonably Achievable

(ALARA).

b. Observations and Findinas

The inspectors review of the licensee's ALARA program determined that

the licensee had established an annual exposure goal of approximately

286 person-rem, which included the Unit 2 outage goal of 132 person-rem

and Jart of a planned Unit 1 outage to begin late in 1997.

At the time

of t1e inspection the licensee was tracking approximately 9 person-rem

below previous estimates. The licensee had continued to track and trend

outage exposures for purposes of future outage preplanning and it was

determined that exposures continue to trend downward based on ALARA

initiatives.

Several ALARA initiatives reviewed during the inspection

that attributed to lower personnel exposures included: improved

scheduling to optimize the use of shielding and reduce worker congestion

in areas; replacement of stellite valve components with components made

from low to no stellite materials: a successful crudburst during the

Unit 2 shutdown which reduced Unit 2 dose rates by approximately 15

percent lower than previous Unit 2 outages; increased use of shielding:

and a improved method for workers to initiate ALARA suggestions.

During tours of the facility the inspectors also observed Radiation

.

protection (RP) technicians controlling access to work areas to minimize

Personnel exposure and briefing workers in the work areas as

radiological conditions changed.

The inspectors also observed personnel

beir.g briefed on ALARA considerations during specific briefings

conducted to address RWP requirements.

c. Conclusions

,

Based on licensee planning efforts to reduce source term and the

licensee's efforts to achieve established exposure goals which were

challenging, the inspectors determined the licensee was maintaining

programs for controlling exposures ALARA and continued to be effective

j

in controlling overall collective dose.

R5

Staff Training and Qualification in Radiation Protection

j

a. Insoection Scoce (83750 and 84750)

,

Training was reviewed to determine whether radiation protection

technicians had been instructed in radiation procedures to minimize

,

radiation exposures and control radioactive material as required by 10

'

CFR 19.12.

t

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b. Observations and Findinas

The inspectors reviewed training requirements for RP technicians and the

4

continuing training curriculum for the period of January 1,1996.

Enclosure 2

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through April 5, 1997, which included industry events and topics to

minimize radiation exposure.

The inspectors also interviewed RP

personnel and observed work practices to determine the effectiveness of

continuing training.

i

c. Conclusions

Based on the training activities reviewed, the inspectors determined

radiation protection technicians were receiving an appropriate level of

training to perform routine work activities involving radiation and/or

radioactive material.

R7

Quality Assurance in Radiation Protection and Chemistry

a. Insoection Scooe (83750)

10 CFR 20.1101 requires that the licensee periodically review the RP

program content and implementation at least annually.

Licensee periodic

reviews of the RP program were reviewed to determine the edequacy of

identification and corrective actions.

'

b. Observations and Findinas

.

By reviewing RP procedures, observing work, reviewing industry

documentation, and performing plant walkdowns to include surveillance of

work areas by supervisors and technicians during normal work coverage,

the inspector determined that Quality Assurance audits and Self-

Assessment efforts in the area of RP were accomplished.

Documentation

of problems by licensee representatives was included in Quality

Assurance Audits and Self-Assessment Reports.

Corrective actions were

included in the licensee's Problem Investigative Process and were being

completed in a timely manner.

During the inspection, the inspector reviewed the licensee's self-

assessment processes for evaluating an event in which unsuspected resin

was found in the 2B containment spray heat exchanger on April 10, 1997.

The resin was analyzed by gamma isotopic analysis and determined to be

mixed bed resin.

The licensee began immediate followup actions to

determine the extent of a Jotential spread of resins into plant systems

that could be affected.

T1e licensee formed a Failure Investigation

Process Team to determine the source of the resin and to develop a

recovery plan.

The team was divided into key areas to identify the root

cause, evaluate sluicing operations and alignments that could affect the

potential spread of resin, identify potentially degraded ecuipment.

identify components that could be potentially impacted, anc develop a

cleanup plan.

The licensee's investigation revealed that the probable

,

'

source of the resin was a potential tear in a screenwire used to contain

!

mixed resin inside of an ion exchanger. The ion exchanger is used

'

during spent fuel pool cleanup evolutions. The licensee determined that

i

only a small amount of resin was present in the containment spray

Enclosure 2

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system, and cleanup actions were initiated to remove the resin that had

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been identified. A total of approximately 200 - 250 milliliters of

o

resin was removed from the spent fuel pool purification and containment

!

spray systems.

The licensee initiated actions to clean out ion

6

<

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exchanger post filter housings whenever filters are changed to help

i

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eliminate the potential for the small amounts of resin from entering

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into the containment s] ray system. The licensee's engineering

'

evaluation concluded tlat there were no operability concerns resulting

.

from this event, and the inspector concluded that the licensee's review

i

l

for operability was logical.

The inspector determined that the licensee

!

was aggressive in performing a root cause analysis of the resin event.

!

!

l

and the licensee's assessments of the event were good.

i

!

c. Conclusions

i

!

The inspector determined the licensee was performing Quality Assurance

!

Audits and effectively assessing the radiation protection program as

required by 10 CFR Part 20.1101. The inspector also determined the

licensee was completing corrective actions in a timely manner.

l

F2

Status of Fire Protection Facilities and Equipment

'

f

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F2.1 00erability of Fire Protection Facilities and Ecuioment

a. Inspection Scoce (64704)

i

i

The inspectors reviewed open corrective maintenance work orders on fire

'

protection components and operation's list of out-of-service fire

protection equipment to assess the licensee's performance for returning

degraded fire protection components to service.

In addition, walkdown

!

inspections were made to assess the material condition of the plant's

l

fire protection systems, equipment, features and fire brigade equipment.

t

b.

Observations and Findinos

!

Maintenance and Ooerability of Fire Protection Ecuioment and Comoonents

l

As of March 31, 1997, there were approximately 22 fire protection

)

related work requests-in which the work had not been completed. Most of

these involved minor corrective maintenance work items and did not

' i'

!

affect the operability of the components.

All of these work requests.

i

except for work request item 910001140, were initiated in 1997 or late

1996.

Item 910001140 involved repairs to the fire pump suction screens

which were to be corrected by minor modification CE-3197. This work had

!

been completed except for the proper reinstallation of the suction

screens.

As of the date of this inspection, these screens had not been

,

i

fully installed to the botsom of the screen frame.

This resulted in an

!

estimated area approximately 78x11 feet in size near the bottom of the

pump suction pit not being filtered.

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Two of the three fire pumps take suction from the fire protection

suction pit.

This suction pit was provided with two suction screens

with 3/8-inch mesh installed to filter and prevent raw lake water trash

and debris from entering the suction pit for the pumps and clogging the

suction inlets for the two pumps.

The third fire pump takes suction

from the suction pit for the low pressure service water pumps.

The fire pump suction screens were found degraded in late 1990 and

repairs were initiated in 1991.

Following these repairs. the suction

'

screens were not properly reinstalled.

Reportedly, a lifting beam

device was misplaced during the modification process.

Without the beam

device the filters could not be properly installed.

The Catawba Fire

Protection OA Program has been incorporated into the Duke Topical Report

GA Program as OA Condition 3.

The Topical Report. Section 17.3.1.6

states that Duke has established a corrective action process whereby all

i

personnel are to assure conditions adverse to quality are promptly

identified, controlled, and corrected. Also. Topical Report Section

17.3.2.13 - Corrective Action. requires conditions adverse to quality to

be corrected

The failure to correct the degraded filter screens for

the fire pumps in a timely manner is identified as Violation 50-

413.414/97-07-05.

Following this inspection, the licensee notified the

inspectors that these screens were properly installed on May 14. 1997.

.

Otherwise, the inspectors concluded that there was no significant

maintenance backlog associated with fire protection components.

Also, as of March 31. 1997, there were 22 degraded or inoperable fire

protection components.

Most of these items were related to the Unit 2

refueling outage which was in progress.

For example several fire

barrier penetrations were open for movement of materials through open

floor hatches and the CO system for the 2A diesel generator was removed

2

from service due to maintenance work being performed on the diesel

engine. The remaining degraded features were either in nonsafety-

related areas or were minor discrepancies which did not affect the

operability of the system or component.

Four of these items had been

degraded since late 1996. the remainder had been degraded since early

1997

The inspectors verified that appropriate com)ensatory measures

had been implemented for the degraded components, w1ere required.

One

degraded component required a continuous fire watch and three degraded

'

components required an hourly fire watch patrol. The remaining degraded

components were considered operable and did not require any compensatory

actions.

'

The inspectors toured the plant and noted that the operable fire

protection systems were well maintained and the material condition was

very good.

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Fire Briaade Eauioment:

The fire brigade turnout gear was stored in a fire brigade equipment

building adjacent to the Unit 2 Turbine Building. A sufficient number

,

of turnout gear, consisting of coats, Sants boots, helmets, etc., was

provided to equip the fire brigade mem)ers expected to respond in the

i

event of a fire or other emergency. The equipment was properly stored

'

and well maintained.

c.

Conclusions

The low number of open maintenance work orders and degraded fire

protection components, in conjunction with the good material condition

of the fire protection components and fire brigade equipment, indicated

that, in general, appropriate em)hasis had been placed on the

maintenance and operability of tie fire protection equipment and

components.

The work to repair the suction screens for two of the three fire pump's

suction piping had been o)en since 1991 and was not complete. The lack

of prompt resolution of t1e work was identified as a violation.

F2.2 Surveillance of Fire Protection Features and Eauioment

.

a.

Insoection Scone (64704)

The inspectors reviewed the following completed surveillance and test

procedures:

-

IP/0/A/3350/13. Revision Change 0 Retype 5. EFA System Detector

Test Procedure, Data Gathering Panel 10.

Completed January 20,

1997.

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IP/0/A/3350/16. Revision Change 0 Retype 2. EFA System Detector

Test Procedure, Data Gathering Panel 13.

Completed February 6.

1997.

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PT/0/A/4400/01A, Revision Change 0 Retype 32. Exterior Fire

Protection Functional Capacity Test.

Completed January 29, 1996.

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PT/0/A/4400/01S, Revision Change 0 Retype 25. Exterior Fire

Protection System - Raw Water Yard (RY) Fire Protection Flow

(Underground) Periodic Test.

Completed April 9.1996 and December

5, 1996.

The frecuency of selected surveillance test procedures were also

reviewec,

i

Enclosure 2

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b.

Observations and Find 1nas

The completed fire protection surveillance tests reviewed by the

inspectors had been appropriately completed and met the. acceptance

criteria. The test procedures were well written and met the fire

3rotection surveillance requirements of FSAR Chapter 16.9. Selected

_icensee Commitments (SLC). The surveillance procedures for the

capacity tests on the fire pumps required test data for multiple points

j

on the pump curve to be obtained.

This data provided good verification

of the pump's performance.

During the review of Surveillance PT/0/A4400/01A. the inspectors noted

that the October 1995 surveillance test indicated that the water flow

through the piping system would not deliver adequate fire flows

This

test is conducted every three years and measures the flow of water

through various sections of piping to determine if the system will

'

provide an adequate flow path from the fire pumps to the various

i

sprinkler and hose stations located in the plant to meet the required

l

design head 3ressure and volume requirements.

Following the October

1995 test, t1e system was extensively flushed and retested in April

i

1996. This test found that the system remained deficient.

The flow

tests were performed by isolating the normal loop piping such that the

flow tests were through a single pipe.

The system would provide the

.

required design flow rates as long as the loop flow paths were

maintained in service.

The licensee developed a major pipe cleaning and flushing project

utilizing the " hydro-lase" process which was performed by station

personnel working under the supervision and coordination of a vendor

specialist.

During the pipe cleaning activities several automatic

sprinkler systems and hose stations were required to be removed from

service.

The licensee coordinated this work to require a minim;m number

of systems to be inoperable at any one time.

Appropriate compensatory

actions, consisting of a fire watch with backup fire suppression, were

provided as remedial actions while the required fire suppression systems

'

were inoperable.

Based on the review of the work activities and

interviews with the plant staff, the inspectors concluded that good

coordination and oversight of these activities were provided.

Following

completion of the pipe cleaning activities the underground piping was

retested in December,1996 and was found to be capable of delivering the

required fire flow.

The surveillance requirements for the fire protection systems were

contained in FSAR Chapter 16.9.

The results of the inspector's review

I

of these features is located in Section F3.

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c.

Conclusions

Good surveillance and test procedures were provided for the fire

protection systems and features.

Procedure implementation was

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effective. The coordination of the fire protection water piping

cleaning project was excellent.

F3

Fire Protection Procedures and Documentation

a.

Insoection Scooe (64704)

The inspectors reviewed the following procedures for compliance with the

NRC requirements and guidelines:

-

Nuclear Station Directive 112. Revision 0. Fire Brigade

Organization. Training and Responsibilities

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Site Directive 2.12.5, Revision 3. Control of Combustible

Materials Within the Protected Area

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Site Directive 2.12.6. Revision 3. Fire Protection. Detection and

Barrier Impairment Reporting

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Site Directive 2.12.7. Revision 4. Fire Protection / Detection

!

Remedial Actions

!.

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Site Directive 3.3.9. Revision 1. Hot Work Authorization

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FSAR Chapter 16.9. (Revision dated 1/30/96). Auxiliary Systems

(Fire Protection Systems)

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Prefire Plans. Revision 6. Catawba Prefire Plans 6.1d Procedures

Plant tours were also performed to assess procedure compliance.

b.

Observations and Findinas

The above procedures were the principle procedures issued to implement

the facility's fire protection program.

These procedures contained the

requirements for program administration. controls over combustibles and

i

ignition sources, fire brigade organization and training, and

o)erability requirements for the fire protection systems and features.

,

T1e procedures were well written and met the licensee's commitments to

!

the NRC.

The inspectors performed plant tours a"d noted that, even though the

plant was in a refueling outage, implementation of the site's fire

l

prevention program for the control of ignition sources, transient

l

combustibles, and general housekeeping was good.

The accumulation of

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transient combustible materials and the number of maintenance activities

'

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in process due to the refueling outage were-more than anticipated during

normal plant operations.

However, appropriate fire prevention controls

were being applied to these activities.

Enclosure 2

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FSAR Chapter 16.9. Selected Licensee Commitments. Auxiliary Systems

(Fire Protection Systems) provides the operability and surveillance

requirements for the fire protection systems and components.

The

inspectors compared these requirements to the requirements which were

formerly in the TS. These requirements remained essentially the same,

except for the following testing frequency changes:

fire detectors.

from monthly to annually; fire protection valve alignments, from monthly

to quarterly; and hose station inspection, from monthly to quarterly.

The licensee had recently changed these surveillance inspection

frequencies based on satisfactory results from performance based

,

l

evaluat wis of these systems. The inspectors verified that appropriate

l

10 CFR 50.59 safety evaluations had been performed for these revisions.

,

The trending data on the performance based surveillance inspections were

reviewed and indicated that the reliability of these systems was greater

than 99 percent.

This substantiated the changes made to the

!

surveillance frequency requirements. The operability requirements in

the SLC were adequate.

However, the water supply and fire detection

systems were the only systems which had time limits established for

restoring inoperable components to operable status. This issue is being

evaluated further by the NRC and is identified as an Inspector Followup

Item pending completion of this review. IFI 50-413.414/97-07-06: Time

Limits for Restoration of Inoperable Fire Protection Components.

.

The prefire plans reviewed by the inspectors were found to be

satisfactory.

A minor modification was in process to relocate and

remove some of the fire extinguishers presently installed within the

.

plant. Also, a standard fire protection water supply system was

scheduled to be installed by late 1991 for the nuclear service water

'

intake pumping structure.

The prefire plans were scheduled to be

revised upon completion of these modifications.

In the interim.

controlled copies of the prefire plans had been marked to indicate the

plant changes as they were completed for each plant area.

c.

Conclusions

The fire protection program implementing procedures were good and met

licensee and NRC requirements.

Implementation of procedures for the

control of ignition sources, transient combustibles, and general

housekeeping was good. An issue regarding time limits for restoration

of inoperable fire protection components will be reviewed further by the

NRC.

F5

Fire Protection Staff Training and Qualification

a.

Inspection Scope (64704)

The inspectors reviewed the fire brigade organization and training

program for compliance with the NRC guidelines and requirements.

l

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Enclosure 2

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b.

Observations and Findinas

[

j

The organization and training requirements for the 31 ant fire brigade

were established by Nuclear Station Directive 112. Revision 0. Fire

i

Brigade Organization. Training and Res]onsibilities. The fire brigade

I

for each shift was composed of a fire arigade leader and at least four

j

brigade members from operations and approximately five members from

maintenance.

The fire brigade leeder was a senior reactor o]erator

(SRO) and was normally one of the unit shift supervisors. T1e other

members from Operations were non-licensed plant operators. One of the

i

!

fire brigade members was normally assigned the duties of fire brigade

safety officer to provide technical and administrative assistance to the

fire brigade leader and to hel) cssure the safe performance of each fire

l

brigade member by checking eac1 member for appropriate dress out prior

to entering the fire area, maintaining records of each fire brigade

l

,

l

exposure to fire or radiatinn hazards, use of self contained breathing

apparatus, and reviewing the prefire plans during the emergency for

'

assurance that appropriate measures are being followed for compliance

l

with applicable safety and fire hazards in the area. Assignment of a

'

l

fire brigade safety officer was identified as a program strength.

l

Each fire brigade member was required to receive initial, quarterly and

annual fire fighting related training and to satisfactorily complete an

.

annual medical evaluation and certification for participation in fire

brigade fire fighting activities.

In addition each member was required

i

to participate in at least two drills per year.

.

As of the date of this inspection, there were a total of 34 operations

trained fire brigade leaders and 73 operations personnel and 29

maintenance personnel on the plant's fire brigade. Approximately 6 fire

brigade leaders.12 operations fire brigade members and 5 mintenance

fire brigade members were assigned to each of the five operations crews.

This was a sufficient number of personnel to meet the facilities fire

brigade procedure requirements for one team leader and nine members per

l

shift.

The inspectors reviewed the training and medical records for the fire

brigade members and verified that the training and medical records were

up to date.

The facility utilized off-site qualified state certified

fire brigade training instructors and a state fire training facility to

perform the annual fire brigade training and practical fire training

,

i

scenarios.

During this inspection, the inspectors witnessed a fire brigade drill

involving a simulated fire in an electrical motor for a component

cooling pump located on the 560 foot elevation of the auxiliary

building.

The response of the fire brigade to the simulated fire was

excellent. The brigade leader's direction and fire brigade members'

i

performance, especially the safety officer, were outstanding.

A

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critique to discuss the brigade performance and future enhancements was

'

held following the drill.

,

c.

Conclusions

The fire brigade organization and training met the requirements of the

site procedures.

Performance by the fire brigade during a drill was

excellent.

The use of the fire brigade safety officer position during

fire emergencies was identified as a program strength.

F6

Fire Protection Organization and Administration

i

a.

Insoection Scooe (64704)

]

The licensee's managemerit and administration of the facilities fire

protection program were reviewed for compliance with the commitments to

the NRC and to current guidelines.

b.

Observations and Findinas

The Civil. Electrical. Reactor. Nuclear Engineering Manager was assigned

the responsibility for implementing the facility's fire protection

program. An engineer was assigned the task of coordinating the entire

,.

fire 3rotection program and for coordinating the maintenance,

opera)ility and modifications on the fire suppression systems, fire

barriers, and fire barrier penetrations.

Another engineer was

i

responsible for coordinating the maintenance, o)erability and

modifications on the fire detection systems.

T1e Manager of Safety

Assurance was responsible for providing appropriate training for the

facility fire brigade and for providing guidance and support in the

'

implementation of the facility's fire protection program.

Support on

generic fire 3rotection issues was provided to the site by an engineer

assigned to t7e Corporate Nuclear Engineering Division.

A corporate Fire Protection Business Excellence Steering Team (BEST).

composed of representatives from each of the three Duke nuclear plants

and the corporate staff, was meeting monthly to discuss fire protection

issues and im)rovements needed to enhance the fire protection program at

each site.

T1e inspectors reviewed the minutes for the first three

meetings in 1997 and noted a number of issues were under consideration

which, if im)lemented should improve the overall fire protection

program at t1e Duke facilities.

The inspector concluded that these

meetings were a positive element of the facility's fire protection

program.

c.

Conclusions

Strong coordination and oversight were provided over the facility's fire

-

protection program.

The Fire Protection BEST was a positive factor in

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the identification of potential problems and in the development and

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implementation of enhancements to the fire protection program.

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F7

Quality Assurance in Fire Protection Activities

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a.

Insoection Scooe (64704)

The following audit report was reviewed:

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Audit SA-95-24(CN)(RA). Triennial Fire Protection Audit conducted

May 15 through June 8, 1995

b.

Observations and Findinas

Audit SA-95-24(CN)(RA) was a triennial 0A audit of the facilities' fire

protection program.

The licensee informed the inspectors that this was

the only comprehensive audit of the fire protection program performed

since Duke's December 18, 1991, request to use performance based

criteria for establishing auoit frequencies was approved by the NRC.'s

letter dated May 7. 1992.

Previously, the TS had required annual,

biannual and triennial audits of the fire protection program.

However,

based on the licensee's assessment of good fire protection performance.

only this one triennial audit had been performed at Catawba in recent

.

years.

TS 6.5.2.9 identified a number of site audits which were performed under

the cognizance of the Nuclear Safety Review Board.

The licensee's

December 18, 1991, letter indicated that the audit frequency for all of

these audits were deleted from the TS. and the OA Topical report was to

be revised to indicate that the " audits of selected aspects of

operational phase activities are performed with a frequency commensurate

with safety significance and in such a manner as to assure that an audit

of all safety related functions is completed within a period of two

years." The OA topical report was revised, but only requires an audit

of all "0A Condition 1 functions" to be completed within a period of two

years. Many of the audit items listed by TS Section 6.5.2.9 are

classified as OA Condition 2 or 3 functions.

The specified time for

these audits are not listed in the OA topical report. The inconsistency

of not providing a specified frequency for Condition 2 and 3 functions

is being further reviewed by the NRC and is identified as Inspector

Follow-up Item pending completion of this review. 50-413.414/97-07-07:

Audit Frequency Requirements for Activities other than OA Condition 1

Functions.

The inspectors reviewed the audit findings from the 1995 OA report and

the corrective actions taken on the identified discrepancies. The

report indicated that a comprehensive audit had been performed with nine

findings identified.

The corrective action on each finding had been

completed in a timely manner.

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c.

Conclusions

The 1995 audit and assessment of the facility's fire protection program

was comprehensive and appropriate corrective action was promptly taken

to resolve identified issues. An issue regarding the control of 0A

audit frequencies will be reviewed further by the NRC.

F8

MiscellaneousFireProtectjonIssues

F8.1 Fire Protection Related NRC Information Notices

The inspector reviewed the licensee's evaluation for the following NRC

Information Notices (IN):

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IN 92-18. Potential loss of Shutdown Capacity During a Control

Room Fire

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IN 92-28. Inadequate Fire Suppression System Testing

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IN 93-41. One Hour Fire Endurance Tests Results For Thermal

Ceramics. 3M Company FS 195'and 3M Company E-50 Interam Fire

,

Barrier Systems

..

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IN 94-28. Potential Problems with Fire Barrier Penetration Seals

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IN 9--31. Potential Failure of WILCO. LEXAN-Type HN-4-L. Fire Hose

Nozzles

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IN 94-58. Reactor Coolant Pump Lube Oil Fire

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IN 95-36. Emergency Lighting

The licensee's evaluations and corrective actions for these ins were

appropriate, except the evaluation documentation for some of the ins did

not fully indicate the results of the evaluations which were actually

performed.

V. Manaaement Meetinos

X1

Exit Meeting Summary

The inspectors ) resented the inspection results to members of licensee

management at t1e conclusion of the inspection on April 30. 1997.

On May 14

a teleconference was held between Region II DRS management and licensee

management representatives to discuss the violation included with this report.

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The licensee acknowledged the findings presented.

No proprietary information

was identified.

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PARTIAL LIST OF PERSONS CONTACTED

Licensee

Bhatnager,

A., Operations Superintendent

Birch. M., Safety Assurance Manager

Christopher. S. , Emergency Planning Supervisor

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Copp. S Nuclear Regulatory Affairs Manager

Coy. S., Radiation Protection Manager

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Forbes. J.,

Engineering Manager

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Giles, R.

Work Control Inservice Inspection Coordination

,

Harrall. T.

Instrument and Electrical Maintenance Superintendent

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Kelly. C.. Maintenance Manager

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Kimball. D., Safety Review Group Manager

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Kitlan. M., Regulatory Compliance Manager

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Kulla

D.

Civil Engineering Supervisor

McCollum

W., Catawba Site Vice-President

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Nicholson. K., Compliance Specialist

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Peterson. G., Station Manager

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Propst. R., Chemistry Manager

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Purser, M.. Senior Engineer

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Robinson

G., Work Control Execution Support

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Rogers

D., Mechanical Maintenance Manager

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Tower, D., Compliance Engineer

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INSPECTION PROCEDURES USED

IP 37550:

Engineering

IP 37551:

Onsite Engineering

IP 40500:

Effectiveness of Licensee Controls in Identifying, Resolving, and

Preventing Problems

IP 49001:

Inspection of Erosion / Corrosion Monitoring Programs

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IP 61726:

Surveillance Observation

IP 62001:

Boric Acid Program Prevention Program

IP 62707:

Maintenance Observation

IP 64704:

Fire Protection Program

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IP 71707:

Plant Operations

IP 71750:

Plant Support Activities

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IP 73753:

Inservice Inspection

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IP 83750:

Occupational Radiation Exposure

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IP 84750:

Radioactive Waste Treatment and Effluent and Environmental

Monitoring

IP 92901:

Followup - Operations

IP 92902:

Followup - Maintenance

IP 92903:

Followup - Engineering

ITEMS OPENED, CLOSED, AND DISCUSSED

.

Opened

50-414/97-07-01

VIO

OPEN

Inadequate Procedure Resulting in

Loss of Spent Fuel Pool Cooling with

Core Off-loaded. (Section 01.1)

50-413,414/97-0? 32

1FI

OPEN

Boron Dilution Mitigation System

Reliability Resolution. (Section

01.4)

50-413.414/97-07-03

IFI

OPEN

Review Corrective Actions For

Storage and Handling Assessment

Findings. (Section M1.2)

50-413,414/97-07-04

NCV

OPEN

Failure to Source Check Survey

Instruments as required by licensee

procedure. (Section R1.1)

50-413.414/97-07-05

VIO

OPEN

Failure to Repair Degraded Suction

Screen Filters for Fire Pumps in a

Timely Manner. (Section F2.1)

50-413,414/97-07-06

IFI

OPEN

Time Limits for Restoration of

Inoperable Fire Protection

,

Components. (Section F.3)

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50-413.414/97-07-07

IFI

OPEN

Audit Frequency Requirements for

Activities other than OA Condition 1

Functions. (Section F.7)

Closed

50-413.414/94-13-01

VIO

CLOSED

Failure to follow Procedure NSD 703

and Station Directive 34.0.5

requirements.

(Section 08.1)

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50-413/95-07-01

VIO

CLOSED

Inadequate Modification Procedure

Resulting in Loss of RHR. (Section

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08.2)

50-413.414/95-07-02

VIO

CLOSED

Inadequate Valve Verification

Activities - Two Examples. (Section

08.3)

50-413.414/96-13-04

VIO

CLOSED

Inadequate Design Controls (MSIV

Solenoid Valves). Standby Shutdown

System Makeup Pump Sizing

Calculation (Section E8.1)

50-413.414/92-01-06

DEV

CLOSED

Breaker Coordination (Section E8.2)

.

50-413.414/96-12-03

VIO

CLOSED

Inadequate Design Controls For

Ensuring Containment Crane Wall and

Floor Drain Screens Implemented

Design Requirements (Section E8.3)

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LIST OF ACRONYMS USED

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ALARA -

As Low As Reasonably Achievable

ANSI

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American Nuclear Standards Institute

ASME -

American Society of Mechanical Engineers

BDMS -

Boron Dilution Mitigation System

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CA

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Auxiliary Feedwater (system)

CHEC -

Designation for EPRI computer code

CFR

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Code of Federal Regulations

DEV

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Deviation

DG

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Diesel Generator

DPC

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Duke Power Company

EFA

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Fire Detection System

EPRI

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Electric Power Research Institute

ESS

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Electric System Support

FAC

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Flow Accelerated Corrosion

FME

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Foreign Material Exclusion

FSAR -

Final Safety Analysis Report

FWST -

Refueling Water Storage Tank

2

ft

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Square Feet

ft-lb -

foot-pounds (force)

GL

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Generic Letter

IFI

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Inspector Followup Item

.

IN

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Information Notice

IR

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Inspection Report

ISI

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Inservice Inspection

MOV

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Motor Operated Valve

MSIV -

Main Steam Isolation Valve

NCV

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Non Cited Violation

NDE

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Nondestructive Examination

NI

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Nuclear Safety Injection (system)

NSD

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Nuclear System Directive

NSM

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Nuclear Station Modification

NRC

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Nuclear Regulatory Commission

OAC

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Operator Aid Computer

PCE

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Personnel Contamination Event

PIP

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Problem Investigation Process

PORV -

Power Operated Relief Valve

psig -

Pounds Per Square Inch Gauge

QA

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Quality Assurance

RCA

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Radiologically Controlled. Area

RCP

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Reactor Coolant Pump

RCS

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Reactor Coolant System

RHR

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Residual Heat Removal

RP

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Radiation Protection

revolutions per minute

rpm

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RWP

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Radiation Work Permits

SG

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Steam Generator

SI

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Safety Injection

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SLC

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Select Licensee Commitments

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SSS

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Standby Shutdown System

TEPR -

Top Equipment Problem Resolution

TS

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Technical Specifications

UFSAR -

Updated Final Safety Analysis Report

VIO

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Violation

VN

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Variation Notice

WO

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Work Order

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