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#REDIRECT [[IR 05000321/1985034]]
{{Adams
| number = ML20140C788
| issue date = 01/14/1986
| title = Insp Repts 50-321/85-34 & 50-366/85-34 on 851110-1220. Violation Noted:Inadequate Procedure Resulting in Isolation of Shutdown Cooling During Refueling Operations & Backseated Valve Not Meeting Tech Spec Limits
| author name = Garner L, Holmesray P, Nejfelt G, Panciera V, Ponciera V
| author affiliation = NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
| addressee name =
| addressee affiliation =
| docket = 05000321, 05000366
| license number =
| contact person =
| document report number = 50-321-85-34, 50-366-85-34, NUDOCS 8601280402
| package number = ML20140C756
| document type = INSPECTION REPORT, NRC-GENERATED, INSPECTION REPORT, UTILITY, TEXT-INSPECTION & AUDIT & I&E CIRCULARS
| page count = 6
}}
See also: [[see also::IR 05000321/1985034]]
 
=Text=
{{#Wiki_filter:)
                    /
  '
          o                                UNITED STATES
  [p KEc ,bo                      NUCLEAR REGULATORY COMMISSION
g'          ',                                REGloN 11
y.            j                        101 MARIETTA STREET, N.W.
*              g                        ATLANTA, GEORGI A 30323
%..../
Report Nos.:      50-321/85-34 and 50-366/85-34
  Licensee: Georgia Power Company
              P. O. Box 4545
              Atlanta, GA 30302
Docket Nos..      50-321 and 50-366                          License Nos.: DPR-57 and NPF-5
  Facility Name:      Hatch 1 and 2
  Inspection Conducted:      November 10 - December 20, 1985
  Inspectors:        [M~                  I
              P. Holmes-Ray, Seniorgsidfift'IHspector
                                                                                    /MM
                                                                                ' Dafd Signed
                        $n                                                  lkY$A
              G.M.Nejfelt,ResiftI[pector                                    ~~ Date' Signed
              )f*fnJA
              L.
                                          L
                    . Eu i e r , ~ esidpsf.Ir[ect5r
                                                                                    Jes'Signed
                                                                                //Dat'e'
Approved by: Y .{          np
                V. W.'Pa Wiera, Section Chief
                                                                                  /Dat
                                                                                    /Yff6
                                                                                        Signed
                Division of Reactor Projects
                                              SUMMARY
Scope:    This inspection involved 236 inspector-hours on site in the areas of
Technical      Specification compliance, operator performance, overall plant
operations, quality assurance practices, station and corporate management
practices, corrective and preventive maintenance activities, site security
procedures, radiation control activities, refueling (Unit 1), and surveillance
activities.
Results:    Of the areas inspected, three violations were identified.                      An
  inadequate procedure resulting in isolation of shutdown cooling during refueling
operations (Unit 1), an improperly performed procedure resulting in inadvertent
isolation of the Reactor Core Isolation Cooling (RCIC) steam line with Unit 2 at
rated conditions, and in Unit 2, a backseatea valve which could not meet
Technical Specification (TS) closing requirements (see paragraphs 5 and 7).
                                                                                                I
                    9601280402 860115
                                                                                                '
                    PDR    ADOCK 05000321
                    O                    PDR
                                                                              .
 
                                        .-      -          .-.
      .
.
                                  REPORT DETAILS
1.  Persons Contacted
    Licensee Employees
    H. C. Nix, Site General Manager
  *T. Greene, Deputy Site General Manager
  *H. L. Summer, Operations Manager
  *T. Seitz, Maintenance Manager
  *C. T. Jones, Engineering Manager
  *R. W. Zavodoski, Health Physics and Chemistry Manager
    P. E. Fornel, Site 0.A. Manager
  *S. B. Tipps, Superintendent of Regulatory Compliance
    Other licensee employees contacted included technicians, operators, security
    force members, and office personnel.
  " Attended exit interview
2.  Exit Interview
    The inspection scope and findings were summarized on December 20, 1985, with
    those persons indicated in paragraph 1 above. During the reporting period      l
    frequent discussions were held with the General Manager and/or his
    assistants concerning inspection findings. The licensee acknowledged the
    findings and took no exception.        The licensee did not identify as    -
    proprietary any of the materials provided to or reviewed by the inspectors
    during this inspection.
3.  Licensee Action on Previous Findings
    The following items have been reviewed by the inspectors and are considered
    resolved.      >
    a.    (Closed) Violation (321/85-02-01) - Startup of Unit I with one
          Automatic Depressurization System (ADS) valve inoperable,
    b.    (Closed) Violation (321/85-02-02) - Procedures not adhered to.
    c.    (Closed) Violation (321,366/85-09-03) - Personnel' error.
    d.    (Closed) Violation (321,366/85-10-02) - Improper battery surveillance.
    e.    (Closed) Violation (321/85-10-01) - Valve position error.
 
                                                    _        _ _ . .                _
        -
    .
                                                  2
<
      f.    -(Closed) Violation (366/85-18-04) - Nitrogen valves out of position.
      g.      (Closed) Violation (321,366/85-22-02) - Lack of administrative control
              of vendor manuals used in safety related calibration procedures.
      h.      (Closed) Violar. ion (321/85-24-01) - Failure to make a four hour
              notification,
      i.      (Closed) IFI (321,366/85-18-01) - Diesel      lube oil    temperature
            monitoring.
      J.      (Closed) IFI (321,366/85-18-02) - Diesel water jacket limits.
      k.      (Closed) IFI (321,366/85-18-03) - Diesel lube oil level check.
  4. Unresolved Items
      URI 321,366/85-05-06: The inspector reviewed the Final Safety Analysis
      Report (FSAR) and Technical Specifications (TSs) for both Units to detareine
      if the load ratings specified in Hatch procedures for the diesel generator
      operation were correct even though differing from vendor recommendations.
      The ordering data for the diesels was also reviewed. The Unit 1 FSAR does
      not specify load ratings for the diesel generators; but Unit 2 FSAR does,
      and the operating procedures agree with these requirements. Hatch
      procedures were revised to reflect 2850 KW as the upper limit beyond which
      the_ diesel should never be loaded during normal surveillance. This item is
      closed.
      URI 321/84-48-01c      Procedure 42FH-ENG-004 has been issued and contains
      adequate instructions to control the placement of new fuel into the fuel
      pool. Included is the requirement for two persons to independently verify
      that the fuel is placed in its proper location and to document the spent
      fuel storage location in the post-inspection fuel bundle location log. This
      item is closed.
  5. Plant Tours (Units 1 and 2)
      The inspector (s) conducted plant tours periodically during the inspection
      interval to verify that monitoring equipment was recording as required,
      equipment was properly tagged, operations personnel were aware of plant
      conditions, and plant housekeeping efforts were adequate. The inspectors
      also determined that appropriate radiation controls were            properly
      established, critical clean areas were being controlled in accordance with
      procedures, excess equipment or material was stored properly and combustible
-
      material and debris were disposed of expeditiously. During tours the
      inspectors looked for the existence of unusual fluid leaks, piping
      vibrations, pipe hanger and seismic restraint settings, various valve and
      breaker positions, equipment danger tags, component positions, adequacy of
      fire fighting equipment, and instrument calibration dates. Some tours were
'
      conducted on backshifts and/or weekends.
                        -~            .  . - - _ .    .-    _ _ _
                                                                                      . -
 
                                                    .  -                                - _
      .
                                              3
1
        The inspector routinely conduct partial walkdowns of Emergency Core Cooling
i,      Systems (ECCS). Valve and breaker / switch lineups and equipment conditions
        are randomly verified both locally and in the control room.
        During a centrol board walkdown on November 18, 1985, in Unit 2, the
        inspector observed an information tag (2-85-31) which indicated that valve
        2E51-F008 (RCIC inboard steam line isolation valve) had been electrically
        backseated on November 7, 1985. Operating personnel indicated that they
        were not aware of any testing which had been performed to verify that the
        closure time requirement in TS could still be met from the backseated
>
        position.    Valve 1G31-F001 (Reactor Water Cleanup System [RWCU] inboard
        isolation valve) was also tagged on its backseat (tag 1-85-44 of
        September 26, 1985). Upon failure to locate evidence that testing had been
        done from the backseat position, the licensee tested both valves.        Valve
        2E51-F008 tested satisfactorily, however valve IG31-F001 exceeded the time
        specified in TS Table 3.7-1 by four seconds (34 vs. 30 sec.). The valve was
        timed again from its normal open, not backseated, position. On this second
        attempt when the timing was performed in accordance with the surveillance
        procedure, the time was 29 seconds and therefore within specifications. The
        valve was reopened and ' eft off its backseat. The major difference between
        the two tests was that t a first time was determined from when the control
        switch was turned until the fully closed indication was received.        By the
        licensee's surveillance procedure, the method used the second time, the time
        was recorded from the illumination of the closure light (dual indication,
        both open and closed light lit) to the extinguishing of the open light (only
        the closed light lit). Therefore, the normal method used by the licensee
        did not include the breakaway and initial valve movement time.      Failure to
        maintain the RWCU valve, 1G312-F001, in a condition such that the specified
        closure time in TS Table 3.7-1 could be met is a violation (321/85-34-01).
      6. Plant Operations Review (Units 1 and 2)
        The inspectors periodically during the inspection interval reviewed shift
1        logs and operations records, including data sheets, instrument traces, and
        records of equipment malfunctions. This review included control room logs
        and auxiliary logs, operating orders, standing orders, jumper logs and
        equipment tagout records.      The inspectors routinely observed operator
        alertness and demeanor during plant tours.      During normal events, operator
        performance and response actions were observed and evaluated.            The
        inspectors conducted random off-hours inspections during the reporting
        interval to assure that operations and security remained at acceptable
        levels. Shift turnovers were observed to verify that they were conducted in
        accordance with approved licensee procedures.
          "
        Within the areas inspected, no violations or deviations were identified.
      7. Technical Specification Compliance (Units 1 and 2)
        During this reporting interval, the inspectors verified compliance with
        selected Limiting Conditions for Operations (LCOs) and results of selected
        surveillance tests.    These verifications were accomplished by direct
  -.                        __
                                          .-    --                    .
 
  .
                      %
                                          4
    observation  of monitoring instrumentation, valve positions, switch
    positions, and review of completed logs and records.          The licensee's
    compliance with selected LC0 action statements were reviewed on selected
    occurrences as they happened.
    On December 6,  1985, with Unit 1 in the process of being defueled, the
    shutdown cooling mode of the Residual Heat Removal (RHR) system was
    inadvertently isolated, while performing design        change  instruction
    42SP-DCI-009-1S " Terminations for ECCS Loop "G" per DCR 81-138". When link
    CC 80 was opened in panel 1H11, in accordance with procedure
    42SP-DCI-009-15, relay K 30 dropped out causing valve 1E11-F008 to shut
    isolating shutdown cooling. As soon as the valve went shut, the licensee
    realized what had happen and closed the link and reestablished the shutdown
    cooling lineup.    Shutdown cooling was isolated for arproximately eight
    minutes. The licensee reviewed the procedure for the other loop of RHR and
4
    found the same error in that procedure. This inadequate procedure affecting
    a safety system is a violation (321/85-34-02).
    On December 18, 1985, with Unit 2 at rated conditions, the procedure for
    High Pressure Coolant Injection (HPCI) differential pressure instrument
    functional test and calibration, 575V-E41-003-2, was being performed. The
    Instrument and Control (I&C) technician plugged into the RCIC module rather
    than the HPCI module causing valve 2E51-F008 to close, thereby isolating the-
    RCIC steam line.    The error was immediately recognized and the 2E51-F008
    valve was reopened, returning RCIC to its standby lineup. This failure to
    follow procedure is a violation (366/85-34-03).
  8. Physical Protection (Units 1 and 2)
    The inspectors verified by observation and interviews during the reporting
    interval that measures taken to assure the physical protection of the
    facility met current requirements.        Areas inspected included the
    organization of the security force, the establishment and maintenance of
    gates, doors and isciation zones in proper condition, that access control
    and badging was proper, and procedures were followed.
    During this reporting period the licensee issued a unrestricted access badge
    to a person authorized only escorted access. The person gained entry to the
    protected area and the vital area using this badge. The details of this
    event and any enforcement action will be contained in report 321,366/85-36.
  9. Review of Nonroutine Events Reported by the Licensee
    The following Licensee Event Reports (LERs) were reviewed for potential
    generic impact, to detect trends, and to determine whether corrective
    actions appeared appropriate. Events which were reported immediately were
    also reviewed as they occurred to determine that Technical Specifications
    were being met and the public health and safety were of utmost considera-
    tion.  The following LERs are considered closed:
          Unit 1: 85-15, 85-18*, 85-19, 85-22
 
                                .-                -    -      -                  . _ .
    .    -
                                            5
            Unit 2:  84-11, 84-18*, 85-16, 85-18, 85-20, 85-21
,
            *In-depth review performed
    10. Refue',ing (Unit 1)
        During this reporting interval the inspectors verified by observation,
        interviews, and procedure review that the refueling was being conducted in
        accordance with regulations.      Areas inspected included adequacy of
        procedures, inspection of fuel to be reused, Technical Specification
        compliance and refueling floor housekeeping.
        During this reporting interval, Unit I core was unloaded with no major
        problems. Also preparation for recovery of the new fuel bundle, which had
        been-dropped into the fuel pool, continued. The method and procedures have
        been established and the lift expected to take place on December 21, 1985.
        Within the areas inspected, no violations or deviations were identified.
                                                                .
1
                                                                                          0
                                                                                '%
  ,              -                        -
                                              -. ---            e - ,, - - - ,
}}

Revision as of 15:44, 27 October 2020

Insp Repts 50-321/85-34 & 50-366/85-34 on 851110-1220. Violation Noted:Inadequate Procedure Resulting in Isolation of Shutdown Cooling During Refueling Operations & Backseated Valve Not Meeting Tech Spec Limits
ML20140C788
Person / Time
Site: Hatch  Southern Nuclear icon.png
Issue date: 01/14/1986
From: Garner L, Holmesray P, Nejfelt G, Panciera V, Ponciera V
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML20140C756 List:
References
50-321-85-34, 50-366-85-34, NUDOCS 8601280402
Download: ML20140C788 (6)


See also: IR 05000321/1985034

Text

)

/

'

o UNITED STATES

[p KEc ,bo NUCLEAR REGULATORY COMMISSION

g' ', REGloN 11

y. j 101 MARIETTA STREET, N.W.

  • g ATLANTA, GEORGI A 30323

%..../

Report Nos.: 50-321/85-34 and 50-366/85-34

Licensee: Georgia Power Company

P. O. Box 4545

Atlanta, GA 30302

Docket Nos.. 50-321 and 50-366 License Nos.: DPR-57 and NPF-5

Facility Name: Hatch 1 and 2

Inspection Conducted: November 10 - December 20, 1985

Inspectors: [M~ I

P. Holmes-Ray, Seniorgsidfift'IHspector

/MM

' Dafd Signed

$n lkY$A

G.M.Nejfelt,ResiftI[pector ~~ Date' Signed

)f*fnJA

L.

L

. Eu i e r , ~ esidpsf.Ir[ect5r

Jes'Signed

//Dat'e'

Approved by: Y .{ np

V. W.'Pa Wiera, Section Chief

/Dat

/Yff6

Signed

Division of Reactor Projects

SUMMARY

Scope: This inspection involved 236 inspector-hours on site in the areas of

Technical Specification compliance, operator performance, overall plant

operations, quality assurance practices, station and corporate management

practices, corrective and preventive maintenance activities, site security

procedures, radiation control activities, refueling (Unit 1), and surveillance

activities.

Results: Of the areas inspected, three violations were identified. An

inadequate procedure resulting in isolation of shutdown cooling during refueling

operations (Unit 1), an improperly performed procedure resulting in inadvertent

isolation of the Reactor Core Isolation Cooling (RCIC) steam line with Unit 2 at

rated conditions, and in Unit 2, a backseatea valve which could not meet

Technical Specification (TS) closing requirements (see paragraphs 5 and 7).

I

9601280402 860115

'

PDR ADOCK 05000321

O PDR

.

.- - .-.

.

.

REPORT DETAILS

1. Persons Contacted

Licensee Employees

H. C. Nix, Site General Manager

  • T. Greene, Deputy Site General Manager
  • H. L. Summer, Operations Manager
  • T. Seitz, Maintenance Manager
  • C. T. Jones, Engineering Manager
  • R. W. Zavodoski, Health Physics and Chemistry Manager

P. E. Fornel, Site 0.A. Manager

  • S. B. Tipps, Superintendent of Regulatory Compliance

Other licensee employees contacted included technicians, operators, security

force members, and office personnel.

" Attended exit interview

2. Exit Interview

The inspection scope and findings were summarized on December 20, 1985, with

those persons indicated in paragraph 1 above. During the reporting period l

frequent discussions were held with the General Manager and/or his

assistants concerning inspection findings. The licensee acknowledged the

findings and took no exception. The licensee did not identify as -

proprietary any of the materials provided to or reviewed by the inspectors

during this inspection.

3. Licensee Action on Previous Findings

The following items have been reviewed by the inspectors and are considered

resolved. >

a. (Closed) Violation (321/85-02-01) - Startup of Unit I with one

Automatic Depressurization System (ADS) valve inoperable,

b. (Closed) Violation (321/85-02-02) - Procedures not adhered to.

c. (Closed) Violation (321,366/85-09-03) - Personnel' error.

d. (Closed) Violation (321,366/85-10-02) - Improper battery surveillance.

e. (Closed) Violation (321/85-10-01) - Valve position error.

_ _ _ . . _

-

.

2

<

f. -(Closed) Violation (366/85-18-04) - Nitrogen valves out of position.

g. (Closed) Violation (321,366/85-22-02) - Lack of administrative control

of vendor manuals used in safety related calibration procedures.

h. (Closed) Violar. ion (321/85-24-01) - Failure to make a four hour

notification,

i. (Closed) IFI (321,366/85-18-01) - Diesel lube oil temperature

monitoring.

J. (Closed) IFI (321,366/85-18-02) - Diesel water jacket limits.

k. (Closed) IFI (321,366/85-18-03) - Diesel lube oil level check.

4. Unresolved Items

URI 321,366/85-05-06: The inspector reviewed the Final Safety Analysis

Report (FSAR) and Technical Specifications (TSs) for both Units to detareine

if the load ratings specified in Hatch procedures for the diesel generator

operation were correct even though differing from vendor recommendations.

The ordering data for the diesels was also reviewed. The Unit 1 FSAR does

not specify load ratings for the diesel generators; but Unit 2 FSAR does,

and the operating procedures agree with these requirements. Hatch

procedures were revised to reflect 2850 KW as the upper limit beyond which

the_ diesel should never be loaded during normal surveillance. This item is

closed.

URI 321/84-48-01c Procedure 42FH-ENG-004 has been issued and contains

adequate instructions to control the placement of new fuel into the fuel

pool. Included is the requirement for two persons to independently verify

that the fuel is placed in its proper location and to document the spent

fuel storage location in the post-inspection fuel bundle location log. This

item is closed.

5. Plant Tours (Units 1 and 2)

The inspector (s) conducted plant tours periodically during the inspection

interval to verify that monitoring equipment was recording as required,

equipment was properly tagged, operations personnel were aware of plant

conditions, and plant housekeeping efforts were adequate. The inspectors

also determined that appropriate radiation controls were properly

established, critical clean areas were being controlled in accordance with

procedures, excess equipment or material was stored properly and combustible

-

material and debris were disposed of expeditiously. During tours the

inspectors looked for the existence of unusual fluid leaks, piping

vibrations, pipe hanger and seismic restraint settings, various valve and

breaker positions, equipment danger tags, component positions, adequacy of

fire fighting equipment, and instrument calibration dates. Some tours were

'

conducted on backshifts and/or weekends.

-~ . . - - _ . .- _ _ _

. -

. - - _

.

3

1

The inspector routinely conduct partial walkdowns of Emergency Core Cooling

i, Systems (ECCS). Valve and breaker / switch lineups and equipment conditions

are randomly verified both locally and in the control room.

During a centrol board walkdown on November 18, 1985, in Unit 2, the

inspector observed an information tag (2-85-31) which indicated that valve

2E51-F008 (RCIC inboard steam line isolation valve) had been electrically

backseated on November 7, 1985. Operating personnel indicated that they

were not aware of any testing which had been performed to verify that the

closure time requirement in TS could still be met from the backseated

>

position. Valve 1G31-F001 (Reactor Water Cleanup System [RWCU] inboard

isolation valve) was also tagged on its backseat (tag 1-85-44 of

September 26, 1985). Upon failure to locate evidence that testing had been

done from the backseat position, the licensee tested both valves. Valve

2E51-F008 tested satisfactorily, however valve IG31-F001 exceeded the time

specified in TS Table 3.7-1 by four seconds (34 vs. 30 sec.). The valve was

timed again from its normal open, not backseated, position. On this second

attempt when the timing was performed in accordance with the surveillance

procedure, the time was 29 seconds and therefore within specifications. The

valve was reopened and ' eft off its backseat. The major difference between

the two tests was that t a first time was determined from when the control

switch was turned until the fully closed indication was received. By the

licensee's surveillance procedure, the method used the second time, the time

was recorded from the illumination of the closure light (dual indication,

both open and closed light lit) to the extinguishing of the open light (only

the closed light lit). Therefore, the normal method used by the licensee

did not include the breakaway and initial valve movement time. Failure to

maintain the RWCU valve, 1G312-F001, in a condition such that the specified

closure time in TS Table 3.7-1 could be met is a violation (321/85-34-01).

6. Plant Operations Review (Units 1 and 2)

The inspectors periodically during the inspection interval reviewed shift

1 logs and operations records, including data sheets, instrument traces, and

records of equipment malfunctions. This review included control room logs

and auxiliary logs, operating orders, standing orders, jumper logs and

equipment tagout records. The inspectors routinely observed operator

alertness and demeanor during plant tours. During normal events, operator

performance and response actions were observed and evaluated. The

inspectors conducted random off-hours inspections during the reporting

interval to assure that operations and security remained at acceptable

levels. Shift turnovers were observed to verify that they were conducted in

accordance with approved licensee procedures.

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Within the areas inspected, no violations or deviations were identified.

7. Technical Specification Compliance (Units 1 and 2)

During this reporting interval, the inspectors verified compliance with

selected Limiting Conditions for Operations (LCOs) and results of selected

surveillance tests. These verifications were accomplished by direct

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observation of monitoring instrumentation, valve positions, switch

positions, and review of completed logs and records. The licensee's

compliance with selected LC0 action statements were reviewed on selected

occurrences as they happened.

On December 6, 1985, with Unit 1 in the process of being defueled, the

shutdown cooling mode of the Residual Heat Removal (RHR) system was

inadvertently isolated, while performing design change instruction

42SP-DCI-009-1S " Terminations for ECCS Loop "G" per DCR 81-138". When link

CC 80 was opened in panel 1H11, in accordance with procedure

42SP-DCI-009-15, relay K 30 dropped out causing valve 1E11-F008 to shut

isolating shutdown cooling. As soon as the valve went shut, the licensee

realized what had happen and closed the link and reestablished the shutdown

cooling lineup. Shutdown cooling was isolated for arproximately eight

minutes. The licensee reviewed the procedure for the other loop of RHR and

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found the same error in that procedure. This inadequate procedure affecting

a safety system is a violation (321/85-34-02).

On December 18, 1985, with Unit 2 at rated conditions, the procedure for

High Pressure Coolant Injection (HPCI) differential pressure instrument

functional test and calibration, 575V-E41-003-2, was being performed. The

Instrument and Control (I&C) technician plugged into the RCIC module rather

than the HPCI module causing valve 2E51-F008 to close, thereby isolating the-

RCIC steam line. The error was immediately recognized and the 2E51-F008

valve was reopened, returning RCIC to its standby lineup. This failure to

follow procedure is a violation (366/85-34-03).

8. Physical Protection (Units 1 and 2)

The inspectors verified by observation and interviews during the reporting

interval that measures taken to assure the physical protection of the

facility met current requirements. Areas inspected included the

organization of the security force, the establishment and maintenance of

gates, doors and isciation zones in proper condition, that access control

and badging was proper, and procedures were followed.

During this reporting period the licensee issued a unrestricted access badge

to a person authorized only escorted access. The person gained entry to the

protected area and the vital area using this badge. The details of this

event and any enforcement action will be contained in report 321,366/85-36.

9. Review of Nonroutine Events Reported by the Licensee

The following Licensee Event Reports (LERs) were reviewed for potential

generic impact, to detect trends, and to determine whether corrective

actions appeared appropriate. Events which were reported immediately were

also reviewed as they occurred to determine that Technical Specifications

were being met and the public health and safety were of utmost considera-

tion. The following LERs are considered closed:

Unit 1: 85-15, 85-18*, 85-19, 85-22

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Unit 2: 84-11, 84-18*, 85-16, 85-18, 85-20, 85-21

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  • In-depth review performed

10. Refue',ing (Unit 1)

During this reporting interval the inspectors verified by observation,

interviews, and procedure review that the refueling was being conducted in

accordance with regulations. Areas inspected included adequacy of

procedures, inspection of fuel to be reused, Technical Specification

compliance and refueling floor housekeeping.

During this reporting interval, Unit I core was unloaded with no major

problems. Also preparation for recovery of the new fuel bundle, which had

been-dropped into the fuel pool, continued. The method and procedures have

been established and the lift expected to take place on December 21, 1985.

Within the areas inspected, no violations or deviations were identified.

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