IR 05000611/2007008: Difference between revisions
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# | {{Adams | ||
| number = ML20133F601 | |||
| issue date = 07/19/1985 | |||
| title = Notice of Violation from Insp on 850611-0708 | |||
| author name = | |||
| author affiliation = NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II) | |||
| addressee name = | |||
| addressee affiliation = | |||
| docket = 05000335, 05000389 | |||
| license number = | |||
| contact person = | |||
| document report number = 50-389-85-17, NUDOCS 8508080356 | |||
| package number = ML20133F573 | |||
| document type = NOTICE OF VIOLATION OF A REGULATION, TEXT-INSPECTION & AUDIT & I&E CIRCULARS | |||
| page count = 1 | |||
}} | |||
{{IR-Nav| site = 05000611 | year = 2007 | report number = 008 }} | |||
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ENCLOSURE 1 NOTICE OF VIOLATION Florida Power and Light Company Docket No. 50-389 St. Lucie Unit 2 License ."o. NPF-16 The following violation was identified during an inspection conducted on June 11 - July 8,1985. The Severity Level was assigned in accordance with the NRC Enforcement Policy (10 CFR Part 2, Appendix C). | |||
10 CFR 50, Appendix B, Criterion V, as ' implemented by section 5.0 of FP&L Topical Quality Assurance Report, requires, in part, that activities affecting quality be prescribed by documented instructions, procedures and drawings and shall be accomplished in accordance with these instructions, | |||
' procedures and drawing Contrary to the above, plant modifications were performed on Unit 2 in 1984 per plant change / modification (PC/M)-015-283 which added redundant over-current devices to electrical distribution systems to comply with NRC Regulatory Guides 1.63 and 1.75. The addition of these devices resulted in some safety-related relays no longer being testable with the unit at powe On June 26, 1985, an attempt was made to perform Operating Procedure (0P) | |||
2-0400053, Engineered Safeguards Relay Test, for Semi-annual Surveillanc The PC/M did not modify the procedures to prevent testing of certain relay This resulted in a plant transient that almost tripped the reacto This is a Severity Level V violation (Supplement I). | |||
Pursuant to 10 CFR 2.201, you are required to submit to this office within 30 days of the date of this Notice a written statement or explanation in reply | |||
. | |||
including: (1) admission or denial of the alleged violations; (2) the reasons | |||
, for the violations if admitted; (3) the corrective steps which have been taken | |||
: and the results achieved; (4) corrective steps which will be taken to avoid further violations; and (5) the date when full compliance will be achieve Security or safeguards information should be submitted as an enclosure to facilitate withholding it from public disclosure as required by 10 CFR 2.790(d) | |||
or 10 CFR 73.2 ' | |||
' ' | |||
Date: | |||
JUL 191985 | |||
, | |||
f G | |||
}} | |||
Revision as of 21:47, 25 September 2020
| ML20133F601 | |
| Person / Time | |
|---|---|
| Site: | Saint Lucie, Hermes |
| Issue date: | 07/19/1985 |
| From: | NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II) |
| To: | |
| Shared Package | |
| ML20133F573 | List: |
| References | |
| 50-389-85-17, NUDOCS 8508080356 | |
| Download: ML20133F601 (1) | |
Text
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ENCLOSURE 1 NOTICE OF VIOLATION Florida Power and Light Company Docket No. 50-389 St. Lucie Unit 2 License ."o. NPF-16 The following violation was identified during an inspection conducted on June 11 - July 8,1985. The Severity Level was assigned in accordance with the NRC Enforcement Policy (10 CFR Part 2, Appendix C).
10 CFR 50, Appendix B, Criterion V, as ' implemented by section 5.0 of FP&L Topical Quality Assurance Report, requires, in part, that activities affecting quality be prescribed by documented instructions, procedures and drawings and shall be accomplished in accordance with these instructions,
' procedures and drawing Contrary to the above, plant modifications were performed on Unit 2 in 1984 per plant change / modification (PC/M)-015-283 which added redundant over-current devices to electrical distribution systems to comply with NRC Regulatory Guides 1.63 and 1.75. The addition of these devices resulted in some safety-related relays no longer being testable with the unit at powe On June 26, 1985, an attempt was made to perform Operating Procedure (0P)
2-0400053, Engineered Safeguards Relay Test, for Semi-annual Surveillanc The PC/M did not modify the procedures to prevent testing of certain relay This resulted in a plant transient that almost tripped the reacto This is a Severity Level V violation (Supplement I).
Pursuant to 10 CFR 2.201, you are required to submit to this office within 30 days of the date of this Notice a written statement or explanation in reply
.
including: (1) admission or denial of the alleged violations; (2) the reasons
, for the violations if admitted; (3) the corrective steps which have been taken
- and the results achieved; (4) corrective steps which will be taken to avoid further violations; and (5) the date when full compliance will be achieve Security or safeguards information should be submitted as an enclosure to facilitate withholding it from public disclosure as required by 10 CFR 2.790(d)
or 10 CFR 73.2 '
' '
Date:
JUL 191985
,
f G