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{{Adams | |||
| number = ML20134J996 | |||
| issue date = 08/13/1985 | |||
| title = Insp Rept 50-312/85-16 on 850601-0714 & 20-31.No Violation or Deviation Noted.Major Areas Inspected:Operational Safety Verification,Maint,Licensee Event Followup,Safety Features Review & Surveillance Activities | |||
| author name = Eckhardt J, Miller L, Perez G | |||
| author affiliation = NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION V) | |||
| addressee name = | |||
| addressee affiliation = | |||
| docket = 05000312 | |||
| license number = | |||
| contact person = | |||
| document report number = 50-312-85-16, GL-83-28, NUDOCS 8508290543 | |||
| package number = ML20134J990 | |||
| document type = INSPECTION REPORT, NRC-GENERATED, INSPECTION REPORT, UTILITY, TEXT-INSPECTION & AUDIT & I&E CIRCULARS | |||
| page count = 10 | |||
}} | |||
See also: [[see also::IR 05000601/2007014]] | |||
=Text= | |||
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U. S. NUCLEAR REGULATORY COMMISSION | |||
' | |||
, | |||
REGION V- | |||
. Report No.. 50-312/85-16 . | |||
, | |||
. ' Docket.No. 50-312 | |||
' | |||
LbenseNo.DPR-54' | |||
w > | |||
s- . Licensee: Sacramento Municipal Utility District | |||
.P. O. Box 15830 | |||
. | |||
Sacramento, California 95813 | |||
^ | |||
Facility Name: RanchoNecoUnitI | |||
> | |||
, | |||
Inspection at: Herald, California (Rancho Seco Site) | |||
Inspection. Conducted: une 1 u and July 20-31, 1985 | |||
' | |||
, | |||
Inspectors: | |||
J. HU Ec ard | |||
r. | |||
oY Resident Inspector | |||
h | |||
Date Signed | |||
, & 0 | |||
Date Signel | |||
G.. PUPer z, Rem)4 | |||
f Inspector | |||
Approved By: '#17 I )_ | |||
' ' | |||
L. F. e'r Jr. , ftfef | |||
e Date Signed | |||
Reacto Projects Seftion.2 | |||
Summary: | |||
Inspection beteen June 1-July 14 and July 20-31, 1985-(Report No. 50- | |||
- | |||
312/85-16). ' - | |||
' | |||
Areas Inspected: This routine * inspection by the Resident Inspectors involved | |||
' | |||
the areas of operational safety; Verification,' maintenance, licensee event | |||
- | |||
followup, safety features' review, and surveillance activities. During this | |||
inspection, Inspection. Procedures 61726, 62703, 71707, 71710, 92700, 94703, | |||
92704,'and 92706 were covered.' 'This inspection involved 183 hours onsite by | |||
two resident inspe'ctors. | |||
' | |||
Results: Of the areas.. inspected, no violations or deviations were identified. | |||
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8508290543 850814 | |||
) PDN ADOCK 05000312 | |||
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1 DETAILS | |||
1. Persons Contacted , | |||
P. Oubre', Manager of Nuclear Operations | |||
*G. Coward, Plant. Superintendent | |||
*N. Brock, Electrical /I&C: Maintenance Supervisor | |||
H. Canter, QA Engineer | |||
*R.-Colombo, Regulatory Compliance Supervisor- | |||
*S. Crunk, Associate Nuclear Engineer. | |||
*J. Field, Engineering and Quality Control Superintendent | |||
J. Jurkovich, Site Resident Engineer. | |||
F. Kellie, Assistant Chemical and Radiation Superintendent | |||
R. Lawrence, Mechanical Maintenance Supervisor, | |||
~ | |||
- | |||
C. Linkhart, Senior Electrical Engineer | |||
R. Miller, Chemistry and Radiation Protection Superintendent | |||
-S. Redeker, Shift Technical Advisor Supervisor | |||
*R. McQuade, QA Engineer | |||
L. Schwieger, Quality Assurance Director | |||
W. Spencer, Operations Superintendent | |||
Other licensee employees contacted included technicians, operators, | |||
mechanics, security and office personnel. | |||
-* Attended the Exit Meeting on July 31, 1985. | |||
-2. Operational Safety Verification | |||
e | |||
At the start of this report period the licensee was completing the | |||
activities scheduled for their refueling outage which started on March | |||
15, 1985. The plant commenced heatup on June 10, 1985 and reached | |||
criticality on June 14, 1985. Zero and low power physics testing was | |||
performed. On June 18, 1985, reactor power was reduced from fourteen | |||
percent power and cooled down to repair a clogged turbine lube oil line. | |||
Af ter completion of the lube oil system reaintenance, the plant began | |||
heatup on June 23, 1985. The plant was approaching criticality again | |||
when an Unusual Event was declared due to a reactor coolant system leak. | |||
The plant was subsequently brought to cold shutdown, and remained in this | |||
condition throughout the remainder of this report period. The events | |||
surrounding the reactor coolant system leak will be discussed in a future | |||
inspection report (50-312/85-19).' | |||
The inspectors observed control room operations, reviewed applicable | |||
logs, and conducted discussions with control room operators. The | |||
inspectors verified from the control room that the appropriate decay heat | |||
, | |||
removal requirements were being met. Tours of the auxiliary building, | |||
turbine building, and reactor building, including exterior areas, were | |||
made to assess equipment conditions and plant conditions. Also the tours | |||
were made to assess the effectiveness of radiological controls and | |||
adherence to regulatory requirements. The inspectors also observed plant | |||
' housekeeping / cleanliness conditions, looked for potential fire and safety | |||
hazards, and observed security and safeguards practices. | |||
. | |||
No~ violations or deviations were identified. | |||
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3. Facility Staff Changes | |||
On June 21, 1985 the Chemistry and Radiation Protection (CRP) | |||
Superintendent resigned from his position. In the interim, until the | |||
position is filled, the Assistant Chemistry and Radiation Protection | |||
Superintendent has assumed the duties and responsibilities of the CRP | |||
Superintendent. | |||
. | |||
On July 18, 1985 the SMUD Board of Directors announced the selection of i | |||
two new members to the licensee's management staff. These were Messrs. I | |||
Dewey K. Lo'we, selected for Deputy General Manager, and Frank Hahn, | |||
selected for Assistant General Manager for Planning. Mr. Lowe recently | |||
retired as a Major General in the United States Air Force. Mr. Hahn has | |||
recently been the Chief of the Energy Division _for the California | |||
' Department of Water Resources. | |||
The licensee has also announced a temporary position change in the | |||
nuclear training area. The Nuclear Training Superintendent was moved to | |||
a position devoted full time to acquiring a plant specific simulator, and | |||
the Nuclear Training Supervisor has been assigned the duties and | |||
responsibilities of the Nuclear Training Superintendent. | |||
4. Followup on Headquarters Request (Temporary Instruction 2515/67) (Closed) | |||
l The inspectors were requested by NRC Headquarters to review the | |||
~11censee's actions involving a safety issue addressed in IE Information | |||
Notice 83-75, " Improper Control Rod. Manipulation". The notice dealt with | |||
the safety significance of control rod misIositioning | |||
i events, including | |||
plant operation with a mispositioned~ control. rod. | |||
The licensee's procedures and training were reviewed and the following | |||
was identified: | |||
* | |||
Procedures existed for recovery froai a mispositioned rod | |||
* | |||
Procedures existed for verifying rod position when one form of | |||
normal indication is lost | |||
* | |||
Training has been provided fer operators in the proper movement of | |||
control rods, the consequences of improper movement, and the | |||
consequences of operating with a mispositioned rod | |||
It appeared that the licensee has provided the proper procedures and | |||
training to address the safety issue of a misposition control rod. | |||
No violations or deviations were identified. | |||
5. Failure of a Reactor Trip Breaker During Testing (LER 85-06 (Closed)) | |||
On June 5, 1985, while the licensee was performing surveillance and | |||
calibration on the "C" channel of the Reactor Protection System (RPS), | |||
the~ reactor trip breaker (RTB), see Figure 1, failed to trip open when | |||
its undervoltage trip attachment (UVTA) was actuated. The licensee | |||
stopped the test being performed, and observed that the undervoltage (UV) | |||
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.. 3 | |||
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1 | |||
armature was physically _ stuck in the energized condition. The licensee l | |||
proceeded to.the next portion of the surveillance test, actuated the ! | |||
shunt trip device of the RTB, and successfully tripped the RTB. | |||
Therefore, although the RTB had failed to trip with the undervoltage j | |||
condition, the breaker was operable using the shunt trip device. ' | |||
The licensee's design used General Electric (GE) AK-2-25 circuit breakers | |||
* | |||
as RTBs. This design consists of six RTBs which must operate in a i | |||
one-out-of-two-taken-twice logic to remove power from the control rod | |||
drive mechanisms (CRDMs) and release all control rods into the core. | |||
There are two AC breakers and four DC breakers. AC breakers control all i | |||
the- three phase primary power to the control rod drives; two DC breakers l | |||
control the DC power to safety rod groups 1 through 4; and the other DC | |||
breakers controls the DC power to safety rod groups 5 through 8. When | |||
any 2-out-of-4 protective channels trip, all reactor trip module logics | |||
trip, commanding all control rod drive breakers to trip. i | |||
The RTB's utilized both a UVTA and a shunt trip device to trip. | |||
. Automatic actuation of the shunt trip was added as a response to NRC | |||
Generic Letter 83-28. A trip signal interrupts power to the UVTA and | |||
simultaneously applied power to the shunt trip device. During a loss of | |||
power or a low control voltage condition, the UVTAs would trip the RTBs. | |||
The B&W design also utilized a silicon controlled rectifier (SCR) system | |||
to diversely remove power from the CRDMs and cause the plant to scram. ; | |||
Power- to each of the regulating rod groups is provided through two ' | |||
separate sets of SCRs. This power may be interrupted by two separate | |||
methods: (1) open the two upstream AC RTBs that supply holding power to , | |||
the rods via the SCRs; or (2) cut off the control power necessary for the l | |||
SCRs to conduct holding power to the rods. ! | |||
' | |||
On June 6,1985 the inspectors observed a bench check of the RTB that | |||
failed. The licensee was able to trip the breaker several times using | |||
L | |||
' | |||
the UVTA; but it was noted that the trip paddle (see figure 1) appeared j | |||
to be loose. The licensee was able to move the trip paddle over the l | |||
armature and prevent the armature from moving out of the energized | |||
position. This configuration appeared to have simulated the original | |||
? failed condition of June 5, 1985, because the armature, could not engage . | |||
' | |||
the trip paddle when the UVTA was deenergized, llowever, the shunt trip | |||
was able to trip the breaker. The licensee then rotated the trip paddle | |||
to its proper position and was able to trip the breaker using the UVTA. | |||
The licensee's Management Safety Review Committee (MSRC) met the evening i | |||
of June 7, 1985, and decided to functionally test all reactor trip | |||
breakers in accordance with a special test procedure (STP-944) developed, | |||
which incorporated the recommendations of GE Service Bulletin 25-014, | |||
" Generic Preventative Maintenance and Surveillance Instructions for | |||
General Electric AK-2/2-15/25 Reactor Trip Breakers Incorporating | |||
Post-Salem Test and Operating Experience." The testing was performed by | |||
the licensee and observed by representatives from B&W and the GE Service ! | |||
Center in Atlanta, Georgia. | |||
After successful completion of STP-944 it was determined that the | |||
licensee had six operable RTBs and that the cause of the breaker failure | |||
. | |||
1 | |||
_ - _ _ . _ _ | |||
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, | |||
. 4 | |||
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' appeared to be an exce aive armature to rivet gap clearance. The | |||
r armature to rivet gap was determined to be approxiaately .059' inches. | |||
' | |||
' | |||
~The specification range was .001 to .010 inches. The greater armature to | |||
rivet gap has been shown to allow the trip paddle to move freely and | |||
~ | |||
b possibly interfere with the proper operation of the armature. | |||
It appears to date that the excessive armature to rivet gap could have | |||
been caused by vibrations of the breaker during transportation to and | |||
from the GE and B&W facilities. , | |||
The licensee sent the six RTBS and one spare to the GE Service Center at | |||
the commencement of the 1985 refueling outage. The breakers were sent in | |||
response to NRC Generic Letter 83-28 for refurbishment. The breakers, | |||
after completion of the refurbishment, were.sent to B&W to be certified | |||
for seismic and electrical class IE qualifications and for 10 CFR 21 | |||
-considerations. The breakers returned to Rancho Seco and the first | |||
functional testing performed was on June 5, 1985, the day of the failure. | |||
The licensee's investigation into the underlying cause of the failure of | |||
* | |||
the UTVA was extensive. The failed RTB was quarantined and was not | |||
altered, so the licensee was able to identify the probable cause of its | |||
failure. The licensee's performance of STP-944 on the other six RTBs | |||
provided the MSRC with sufficient information to declare the breakers | |||
operable. The licensee also sent a member of their Quality Assurance | |||
department to both the GE Service Center and B&W to observe RTB testing | |||
and to reverify the work performed during breaker refurbishment. | |||
The licensee identified that the GE Service Bulletin recommended the | |||
measurement of the armature to rivet gap, but did not specify the proper , | |||
position of the armature when measured. ? The licensee discovered that GE | |||
technicians'always measured this gap.with the armature in the energized | |||
' | |||
position. . | |||
The licensee'has incorporated.the guidance of the GE Service Bulletin | |||
into their surveillance procedure for- the RTBs. Additionally it appears | |||
that the failure mechanism, excessive armature to rivet gap, has been | |||
' | |||
appropriately identified and the, corrective actions performed | |||
s satisfactorily tested all RTBs | |||
' | |||
'before the licensee began withdrawing | |||
control rods. '' | |||
,,,, | |||
, - | |||
The licensee reported this event in Licensee Event Report (LER) Number | |||
85-06. The inspector verified that reporting requirements had been met, | |||
causes had been identified, corrective, actions appeared appropriate, and | |||
. generic applicability had been considered. 'This LER is closed. | |||
No violations or deviations were identified. | |||
6. Nuclear Service Cooling Water Pump Breaker | |||
The ' A' nuclear service cooling water (NSCW) pump breaker experienced | |||
three trips during the period of June 11-13, 1985. The NSCW system | |||
removes heat from the decay heat removal system. | |||
_ . | |||
. | |||
, | |||
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After each of the first two breaker trips, the breaker was tested, placed | |||
, back into service, and successfully completed'its surveillance test. The | |||
- | |||
results of tests performed did-not provide sufficient information on the | |||
causes for the breaker's actuation.. On June 13, 1985, the licensee | |||
replaced the breaker and initiated bench testing of it. The licensee had' | |||
the vendor troubleshoot'the breaker; at the end of this report period the | |||
vendor's investigation had not conclusively determined the cause of the | |||
trips. | |||
The licensee has appointed a failure investigation team consisting of | |||
three electrical engineers to review this event.. Their investigation was | |||
not completed at the end of this report period. Therefore, this item | |||
remains open for future review of the team's findings (0 pen Item | |||
-85-16-01). | |||
, | |||
During the investigation of the NSCW pump breaker, the licensee | |||
determined that, due to an earlier impeller modification, the pump motor | |||
was drawing current slightly higher than the pump's original rating. | |||
Although the licensee has determined this higher current not to be the | |||
cause of the breaker's trips, a new overload unit setting has been made | |||
for both the A and B train breakers. | |||
No violations or deviations were identified. | |||
7. Reactor Heatup, Startup, and Zero Power Physics Testing | |||
After the ninety day refueling outage, plant heatup commenced on June 12, | |||
1985 and the reactor was brought critical on June 14, 1985. Zero power | |||
physics testing was performed and the plant was taken to 14 percent power | |||
on June 18, 1985. On that date, the plant was shutdown and taken to' cold | |||
shutdown conditions to repair a flow blockage problem in the main turbine | |||
. lubricating oil system. | |||
During this period, the inspectors observed portions of the control room' | |||
activities including plant-heatup, deboration, and physics testing. The | |||
operators were knowledgeable of the plant conditions and were following | |||
applicable procedures. | |||
No violations or deviations were identified. | |||
8. Evaluation of Auxiliary Feedwater System | |||
. Because of a June 9 event at the Davis-Besse facility involving the | |||
auxiliary feedwater (AW) system, the licensee performed an evaluation of | |||
the Rancho Seco AW system to ensure its operability. This evaluat. ion | |||
involved'a review of the latest surveillance testing data, additional | |||
stroke testing'of certain valves, refresher training of all operating | |||
crews regarding a loss of feedwater event, and additional valve lineups | |||
of the AW systems. Additionally, the licensee sent a represent 1tive to | |||
Davis-Besse to obtain first hand information concerning their main | |||
feedwater and AW systems and the events of June 9. The licensee | |||
concluded that there were significant differences between the Rancho Seco | |||
and Davis-Besse AW systems, making the Rancho Seco system much more | |||
reliabic. The inspectors agreed with the licensee's conclusions. The | |||
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. . licensee'is continuing'to evaluate the proposed emergency feedwater | |||
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a > ; initiation and control'_(RFIC)' system with respect to the Davis-Besse | |||
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'* . The following were the' major design' differences between tho's'ystems at - 1 | |||
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,i Rancho Seco and Davis-Besse: ' | |||
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Eta'cho a Seco does not have dedicated main' steam isolation valves. | |||
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'; s(MSIVs).other than.the main'turbine throttie e valves.. ,; | |||
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Actuation of 'the Rancho' Seco main: steam line- break' (MSLB) logic , | |||
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, | |||
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> . control.did not' affect.the valve lineup,of the auxiliary feedwater > | |||
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- system, fas did the. Davis-Besse steam 'and 'feedwater rupture . control ' | |||
system;(SFRCS). gp, | |||
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JRancho Seco had two motor driven ~' auxiliary feed" pumps. one of Ohich. - | |||
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also has a tanden" turbine drive.. Davis-Besse used two turbine. .' | |||
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I. driven auxiliary feed pumps.' ' | |||
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. Rancho Seco' operated'wiEh the.pressuriser electr$natic" relief valve | |||
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u '(EMOV) blocked. q 3 .a | |||
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On June 15 and'16, the inspectors. performed walkdowns;of the AFW system.- | |||
Included in the walkdown wasta valve position check'for each valveu | |||
" | |||
. /- | |||
' ,- identified in the AFW system operating procedure A.51. . The inspectors + | |||
determined that all, valves were positioned as required.1 The following i | |||
, l minor. anomalies were identified ,- | |||
,, 4 | |||
. - | |||
. . , | |||
. , | |||
* | |||
. Vent and drain valves FWS-135 and FWS-136'were not included'in the | |||
' valve line-up. .These valves were located lietween two closed valves | |||
~ | |||
- | |||
, | |||
in the-test line between the AFW pumps and the condenser.. , | |||
* | |||
A. pull box cover was missing on the heat tracing conduit. | |||
' | |||
* | |||
Calibration. stickers for two flow transmitters had the same- * | |||
recalibration dates as the calibration dates. | |||
*- No valve tag was attached to bypass valve FWS-562.' | |||
These minor problems.were immediately corrected by the licensee. t | |||
4 | |||
'In~ addition to'the system walkdowns, the inspectors attended the operator ; | |||
' | |||
' | |||
4 | |||
, | |||
briefings and retraining on the AFW operation, reviewed recent AFW system | |||
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surveillance test data, work requests and outstanding nonconformance | |||
reports to ensure operational readiness. | |||
' | |||
, | |||
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No violations or deviations were identified. | |||
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.. | |||
9. Diesel Generator Control Circuit problen , | |||
After surveillance testing of diesel generator CEA, the bus unloading ; | |||
. system caused the diesel generator output breaker to cycle, with the | |||
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system in the maintenance stop mode because an undervoltage condition ; | |||
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- +_ua..--.-_-. n.---_.._--~-_u- . . . . - - _ ~ _ - - _ _ _ . . . - . _ - _ - . _ . _ - - - _ - | |||
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existed on 4160V Bus S4A2. Bus S4A2 was deenergized for maintenance | |||
during this time. | |||
To prevent the cycling in the future, in the event that an undervoltage | |||
condition would exist during the time the engine was in the maintenance | |||
> stop mode, the 'Licencee has modified the auto-start circuit for both GEA | |||
and GEB diesel generator engine control circuits. Time delay dropout | |||
relays were added in each auto-start circuit to allow the nor.nal shutdown | |||
timer to time out, thus preventing the diesel generator breaker and bus | |||
unloading system from cycling. The new Class IE relays were installed | |||
within panels H2 DEA and H2 DEB. It is noted that this condition would | |||
have been over-ridden if a safety features actuation signal would have | |||
occurred. | |||
The inspectota reviewed the engineering change notice (A-5730) associated | |||
with this modification ind observed the installed new relays. | |||
No violations or deviations were' identified. | |||
10. Meetings with LRS Implementing Committee, MSRC, and SMUD Board of | |||
Directors | |||
During this reporting period, four significant meetings were held with | |||
the licensee's manai nent. | |||
On June l' * | |||
resident inspectors and Region V management met | |||
with the F ectors subcommittee responsible for implementing the | |||
LRS reconune t . at Rancho Seco. The purpose of this meeting was to | |||
discuss the , ugress and status of the implementation of the | |||
recommendations. The NRC took advantage of this meeting to discuss the | |||
need for continuing programs to ensure the recommendations are | |||
implemented and then to evaluate the effectiveness of the implementation. | |||
On July 3 and July 10, 1985, the resident inspectors and Region V | |||
management attended MSRC meetings. The July 10 meeting was also attended | |||
by representatives of I&E and NRR. The purpose of these meetings was to | |||
discuss the vent pipe break event at Rancho Seco (which will be discussed. | |||
In detail in inspection report 85-19) and other recent problems. The | |||
licensee presented their evaluation of the recent events, corrective | |||
action to ensure the problems are corrected, and long term corrective | |||
action. | |||
On July 18, 1985, Region V management and representatives from I&E and | |||
NRR met with the SMUD Board of Directors to discuss the overall | |||
performance of Rancho Seco. Comparisons of the licensee's present | |||
performance with the performance a year ago were made. Areas coverd | |||
were the licensee's concept of rising standards of excellence, technical ' | |||
adequacy, facing facts, respect for radiation, training, responsibility, | |||
and capacity to learn from experience. The licensee was encouraged to | |||
continue with the improving programs that have begun. | |||
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July;31,71985. The scope., and findings of the inspection activities as . | |||
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Revision as of 10:24, 2 September 2020
| ML20134J996 | |
| Person / Time | |
|---|---|
| Site: | Rancho Seco |
| Issue date: | 08/13/1985 |
| From: | Eckhardt J, Miller L, Perez G NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION V) |
| To: | |
| Shared Package | |
| ML20134J990 | List: |
| References | |
| 50-312-85-16, GL-83-28, NUDOCS 8508290543 | |
| Download: ML20134J996 (10) | |
See also: IR 05000601/2007014
Text
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U. S. NUCLEAR REGULATORY COMMISSION
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REGION V-
. Report No.. 50-312/85-16 .
,
. ' Docket.No. 50-312
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LbenseNo.DPR-54'
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s- . Licensee: Sacramento Municipal Utility District
.P. O. Box 15830
.
Sacramento, California 95813
^
Facility Name: RanchoNecoUnitI
>
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Inspection at: Herald, California (Rancho Seco Site)
Inspection. Conducted: une 1 u and July 20-31, 1985
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Inspectors:
J. HU Ec ard
r.
oY Resident Inspector
h
Date Signed
, & 0
Date Signel
G.. PUPer z, Rem)4
f Inspector
Approved By: '#17 I )_
' '
L. F. e'r Jr. , ftfef
e Date Signed
Reacto Projects Seftion.2
Summary:
Inspection beteen June 1-July 14 and July 20-31, 1985-(Report No. 50-
-
312/85-16). ' -
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Areas Inspected: This routine * inspection by the Resident Inspectors involved
'
the areas of operational safety; Verification,' maintenance, licensee event
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followup, safety features' review, and surveillance activities. During this
inspection, Inspection. Procedures 61726, 62703, 71707, 71710, 92700, 94703,
92704,'and 92706 were covered.' 'This inspection involved 183 hours0.00212 days <br />0.0508 hours <br />3.025794e-4 weeks <br />6.96315e-5 months <br /> onsite by
two resident inspe'ctors.
'
Results: Of the areas.. inspected, no violations or deviations were identified.
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1 DETAILS
1. Persons Contacted ,
P. Oubre', Manager of Nuclear Operations
- G. Coward, Plant. Superintendent
- N. Brock, Electrical /I&C: Maintenance Supervisor
H. Canter, QA Engineer
- R.-Colombo, Regulatory Compliance Supervisor-
- S. Crunk, Associate Nuclear Engineer.
- J. Field, Engineering and Quality Control Superintendent
J. Jurkovich, Site Resident Engineer.
F. Kellie, Assistant Chemical and Radiation Superintendent
R. Lawrence, Mechanical Maintenance Supervisor,
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C. Linkhart, Senior Electrical Engineer
R. Miller, Chemistry and Radiation Protection Superintendent
-S. Redeker, Shift Technical Advisor Supervisor
- R. McQuade, QA Engineer
L. Schwieger, Quality Assurance Director
W. Spencer, Operations Superintendent
Other licensee employees contacted included technicians, operators,
mechanics, security and office personnel.
-* Attended the Exit Meeting on July 31, 1985.
-2. Operational Safety Verification
e
At the start of this report period the licensee was completing the
activities scheduled for their refueling outage which started on March
15, 1985. The plant commenced heatup on June 10, 1985 and reached
criticality on June 14, 1985. Zero and low power physics testing was
performed. On June 18, 1985, reactor power was reduced from fourteen
percent power and cooled down to repair a clogged turbine lube oil line.
Af ter completion of the lube oil system reaintenance, the plant began
heatup on June 23, 1985. The plant was approaching criticality again
when an Unusual Event was declared due to a reactor coolant system leak.
The plant was subsequently brought to cold shutdown, and remained in this
condition throughout the remainder of this report period. The events
surrounding the reactor coolant system leak will be discussed in a future
inspection report (50-312/85-19).'
The inspectors observed control room operations, reviewed applicable
logs, and conducted discussions with control room operators. The
inspectors verified from the control room that the appropriate decay heat
,
removal requirements were being met. Tours of the auxiliary building,
turbine building, and reactor building, including exterior areas, were
made to assess equipment conditions and plant conditions. Also the tours
were made to assess the effectiveness of radiological controls and
adherence to regulatory requirements. The inspectors also observed plant
' housekeeping / cleanliness conditions, looked for potential fire and safety
hazards, and observed security and safeguards practices.
.
No~ violations or deviations were identified.
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3. Facility Staff Changes
On June 21, 1985 the Chemistry and Radiation Protection (CRP)
Superintendent resigned from his position. In the interim, until the
position is filled, the Assistant Chemistry and Radiation Protection
Superintendent has assumed the duties and responsibilities of the CRP
Superintendent.
.
On July 18, 1985 the SMUD Board of Directors announced the selection of i
two new members to the licensee's management staff. These were Messrs. I
Dewey K. Lo'we, selected for Deputy General Manager, and Frank Hahn,
selected for Assistant General Manager for Planning. Mr. Lowe recently
retired as a Major General in the United States Air Force. Mr. Hahn has
recently been the Chief of the Energy Division _for the California
' Department of Water Resources.
The licensee has also announced a temporary position change in the
nuclear training area. The Nuclear Training Superintendent was moved to
a position devoted full time to acquiring a plant specific simulator, and
the Nuclear Training Supervisor has been assigned the duties and
responsibilities of the Nuclear Training Superintendent.
4. Followup on Headquarters Request (Temporary Instruction 2515/67) (Closed)
l The inspectors were requested by NRC Headquarters to review the
~11censee's actions involving a safety issue addressed in IE Information
Notice 83-75, " Improper Control Rod. Manipulation". The notice dealt with
the safety significance of control rod misIositioning
i events, including
plant operation with a mispositioned~ control. rod.
The licensee's procedures and training were reviewed and the following
was identified:
Procedures existed for recovery froai a mispositioned rod
Procedures existed for verifying rod position when one form of
normal indication is lost
Training has been provided fer operators in the proper movement of
control rods, the consequences of improper movement, and the
consequences of operating with a mispositioned rod
It appeared that the licensee has provided the proper procedures and
training to address the safety issue of a misposition control rod.
No violations or deviations were identified.
5. Failure of a Reactor Trip Breaker During Testing (LER 85-06 (Closed))
On June 5, 1985, while the licensee was performing surveillance and
calibration on the "C" channel of the Reactor Protection System (RPS),
the~ reactor trip breaker (RTB), see Figure 1, failed to trip open when
its undervoltage trip attachment (UVTA) was actuated. The licensee
stopped the test being performed, and observed that the undervoltage (UV)
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armature was physically _ stuck in the energized condition. The licensee l
proceeded to.the next portion of the surveillance test, actuated the !
shunt trip device of the RTB, and successfully tripped the RTB.
Therefore, although the RTB had failed to trip with the undervoltage j
condition, the breaker was operable using the shunt trip device. '
The licensee's design used General Electric (GE) AK-2-25 circuit breakers
as RTBs. This design consists of six RTBs which must operate in a i
one-out-of-two-taken-twice logic to remove power from the control rod
drive mechanisms (CRDMs) and release all control rods into the core.
There are two AC breakers and four DC breakers. AC breakers control all i
the- three phase primary power to the control rod drives; two DC breakers l
control the DC power to safety rod groups 1 through 4; and the other DC
breakers controls the DC power to safety rod groups 5 through 8. When
any 2-out-of-4 protective channels trip, all reactor trip module logics
trip, commanding all control rod drive breakers to trip. i
The RTB's utilized both a UVTA and a shunt trip device to trip.
. Automatic actuation of the shunt trip was added as a response to NRC
Generic Letter 83-28. A trip signal interrupts power to the UVTA and
simultaneously applied power to the shunt trip device. During a loss of
power or a low control voltage condition, the UVTAs would trip the RTBs.
The B&W design also utilized a silicon controlled rectifier (SCR) system
to diversely remove power from the CRDMs and cause the plant to scram. ;
Power- to each of the regulating rod groups is provided through two '
separate sets of SCRs. This power may be interrupted by two separate
methods: (1) open the two upstream AC RTBs that supply holding power to ,
the rods via the SCRs; or (2) cut off the control power necessary for the l
SCRs to conduct holding power to the rods. !
'
On June 6,1985 the inspectors observed a bench check of the RTB that
failed. The licensee was able to trip the breaker several times using
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the UVTA; but it was noted that the trip paddle (see figure 1) appeared j
to be loose. The licensee was able to move the trip paddle over the l
armature and prevent the armature from moving out of the energized
position. This configuration appeared to have simulated the original
? failed condition of June 5, 1985, because the armature, could not engage .
'
the trip paddle when the UVTA was deenergized, llowever, the shunt trip
was able to trip the breaker. The licensee then rotated the trip paddle
to its proper position and was able to trip the breaker using the UVTA.
The licensee's Management Safety Review Committee (MSRC) met the evening i
of June 7, 1985, and decided to functionally test all reactor trip
breakers in accordance with a special test procedure (STP-944) developed,
which incorporated the recommendations of GE Service Bulletin 25-014,
" Generic Preventative Maintenance and Surveillance Instructions for
General Electric AK-2/2-15/25 Reactor Trip Breakers Incorporating
Post-Salem Test and Operating Experience." The testing was performed by
the licensee and observed by representatives from B&W and the GE Service !
Center in Atlanta, Georgia.
After successful completion of STP-944 it was determined that the
licensee had six operable RTBs and that the cause of the breaker failure
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' appeared to be an exce aive armature to rivet gap clearance. The
r armature to rivet gap was determined to be approxiaately .059' inches.
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~The specification range was .001 to .010 inches. The greater armature to
rivet gap has been shown to allow the trip paddle to move freely and
~
b possibly interfere with the proper operation of the armature.
It appears to date that the excessive armature to rivet gap could have
been caused by vibrations of the breaker during transportation to and
from the GE and B&W facilities. ,
The licensee sent the six RTBS and one spare to the GE Service Center at
the commencement of the 1985 refueling outage. The breakers were sent in
response to NRC Generic Letter 83-28 for refurbishment. The breakers,
after completion of the refurbishment, were.sent to B&W to be certified
for seismic and electrical class IE qualifications and for 10 CFR 21
-considerations. The breakers returned to Rancho Seco and the first
functional testing performed was on June 5, 1985, the day of the failure.
The licensee's investigation into the underlying cause of the failure of
the UTVA was extensive. The failed RTB was quarantined and was not
altered, so the licensee was able to identify the probable cause of its
failure. The licensee's performance of STP-944 on the other six RTBs
provided the MSRC with sufficient information to declare the breakers
operable. The licensee also sent a member of their Quality Assurance
department to both the GE Service Center and B&W to observe RTB testing
and to reverify the work performed during breaker refurbishment.
The licensee identified that the GE Service Bulletin recommended the
measurement of the armature to rivet gap, but did not specify the proper ,
position of the armature when measured. ? The licensee discovered that GE
technicians'always measured this gap.with the armature in the energized
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position. .
The licensee'has incorporated.the guidance of the GE Service Bulletin
into their surveillance procedure for- the RTBs. Additionally it appears
that the failure mechanism, excessive armature to rivet gap, has been
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appropriately identified and the, corrective actions performed
s satisfactorily tested all RTBs
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'before the licensee began withdrawing
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The licensee reported this event in Licensee Event Report (LER) Number
85-06. The inspector verified that reporting requirements had been met,
causes had been identified, corrective, actions appeared appropriate, and
. generic applicability had been considered. 'This LER is closed.
No violations or deviations were identified.
6. Nuclear Service Cooling Water Pump Breaker
The ' A' nuclear service cooling water (NSCW) pump breaker experienced
three trips during the period of June 11-13, 1985. The NSCW system
removes heat from the decay heat removal system.
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After each of the first two breaker trips, the breaker was tested, placed
, back into service, and successfully completed'its surveillance test. The
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results of tests performed did-not provide sufficient information on the
causes for the breaker's actuation.. On June 13, 1985, the licensee
replaced the breaker and initiated bench testing of it. The licensee had'
the vendor troubleshoot'the breaker; at the end of this report period the
vendor's investigation had not conclusively determined the cause of the
trips.
The licensee has appointed a failure investigation team consisting of
three electrical engineers to review this event.. Their investigation was
not completed at the end of this report period. Therefore, this item
remains open for future review of the team's findings (0 pen Item
-85-16-01).
,
During the investigation of the NSCW pump breaker, the licensee
determined that, due to an earlier impeller modification, the pump motor
was drawing current slightly higher than the pump's original rating.
Although the licensee has determined this higher current not to be the
cause of the breaker's trips, a new overload unit setting has been made
for both the A and B train breakers.
No violations or deviations were identified.
7. Reactor Heatup, Startup, and Zero Power Physics Testing
After the ninety day refueling outage, plant heatup commenced on June 12,
1985 and the reactor was brought critical on June 14, 1985. Zero power
physics testing was performed and the plant was taken to 14 percent power
on June 18, 1985. On that date, the plant was shutdown and taken to' cold
shutdown conditions to repair a flow blockage problem in the main turbine
. lubricating oil system.
During this period, the inspectors observed portions of the control room'
activities including plant-heatup, deboration, and physics testing. The
operators were knowledgeable of the plant conditions and were following
applicable procedures.
No violations or deviations were identified.
8. Evaluation of Auxiliary Feedwater System
. Because of a June 9 event at the Davis-Besse facility involving the
auxiliary feedwater (AW) system, the licensee performed an evaluation of
the Rancho Seco AW system to ensure its operability. This evaluat. ion
involved'a review of the latest surveillance testing data, additional
stroke testing'of certain valves, refresher training of all operating
crews regarding a loss of feedwater event, and additional valve lineups
of the AW systems. Additionally, the licensee sent a represent 1tive to
Davis-Besse to obtain first hand information concerning their main
feedwater and AW systems and the events of June 9. The licensee
concluded that there were significant differences between the Rancho Seco
and Davis-Besse AW systems, making the Rancho Seco system much more
reliabic. The inspectors agreed with the licensee's conclusions. The
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'* . The following were the' major design' differences between tho's'ystems at - 1
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Eta'cho a Seco does not have dedicated main' steam isolation valves.
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- system, fas did the. Davis-Besse steam 'and 'feedwater rupture . control '
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JRancho Seco had two motor driven ~' auxiliary feed" pumps. one of Ohich. -
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On June 15 and'16, the inspectors. performed walkdowns;of the AFW system.-
Included in the walkdown wasta valve position check'for each valveu
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' ,- identified in the AFW system operating procedure A.51. . The inspectors +
determined that all, valves were positioned as required.1 The following i
, l minor. anomalies were identified ,-
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. Vent and drain valves FWS-135 and FWS-136'were not included'in the
' valve line-up. .These valves were located lietween two closed valves
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in the-test line between the AFW pumps and the condenser.. ,
A. pull box cover was missing on the heat tracing conduit.
'
Calibration. stickers for two flow transmitters had the same- *
recalibration dates as the calibration dates.
- - No valve tag was attached to bypass valve FWS-562.'
These minor problems.were immediately corrected by the licensee. t
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'In~ addition to'the system walkdowns, the inspectors attended the operator ;
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briefings and retraining on the AFW operation, reviewed recent AFW system
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surveillance test data, work requests and outstanding nonconformance
reports to ensure operational readiness.
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No violations or deviations were identified.
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9. Diesel Generator Control Circuit problen ,
After surveillance testing of diesel generator CEA, the bus unloading ;
. system caused the diesel generator output breaker to cycle, with the
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system in the maintenance stop mode because an undervoltage condition ;
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existed on 4160V Bus S4A2. Bus S4A2 was deenergized for maintenance
during this time.
To prevent the cycling in the future, in the event that an undervoltage
condition would exist during the time the engine was in the maintenance
> stop mode, the 'Licencee has modified the auto-start circuit for both GEA
and GEB diesel generator engine control circuits. Time delay dropout
relays were added in each auto-start circuit to allow the nor.nal shutdown
timer to time out, thus preventing the diesel generator breaker and bus
unloading system from cycling. The new Class IE relays were installed
within panels H2 DEA and H2 DEB. It is noted that this condition would
have been over-ridden if a safety features actuation signal would have
occurred.
The inspectota reviewed the engineering change notice (A-5730) associated
with this modification ind observed the installed new relays.
No violations or deviations were' identified.
10. Meetings with LRS Implementing Committee, MSRC, and SMUD Board of
Directors
During this reporting period, four significant meetings were held with
the licensee's manai nent.
On June l' *
resident inspectors and Region V management met
with the F ectors subcommittee responsible for implementing the
LRS reconune t . at Rancho Seco. The purpose of this meeting was to
discuss the , ugress and status of the implementation of the
recommendations. The NRC took advantage of this meeting to discuss the
need for continuing programs to ensure the recommendations are
implemented and then to evaluate the effectiveness of the implementation.
On July 3 and July 10, 1985, the resident inspectors and Region V
management attended MSRC meetings. The July 10 meeting was also attended
by representatives of I&E and NRR. The purpose of these meetings was to
discuss the vent pipe break event at Rancho Seco (which will be discussed.
In detail in inspection report 85-19) and other recent problems. The
licensee presented their evaluation of the recent events, corrective
action to ensure the problems are corrected, and long term corrective
action.
On July 18, 1985, Region V management and representatives from I&E and
NRR met with the SMUD Board of Directors to discuss the overall
performance of Rancho Seco. Comparisons of the licensee's present
performance with the performance a year ago were made. Areas coverd
were the licensee's concept of rising standards of excellence, technical '
adequacy, facing facts, respect for radiation, training, responsibility,
and capacity to learn from experience. The licensee was encouraged to
continue with the improving programs that have begun.
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July;31,71985. The scope., and findings of the inspection activities as .
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