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{{#Wiki_filter:August 14, 2006Paul D. HinnenkampVice President - Operations
{{#Wiki_filter:August 14, 2006
Paul D. Hinnenkamp
Vice President - Operations
Entergy Operations, Inc.
Entergy Operations, Inc.
River Bend Station
River Bend Station
5485 US Highway 61N
5485 US Highway 61N
St. Francisville, LA
St. Francisville, LA 70775
70775SUBJECT:RIVER BEND STATION - NRC INTEGRATED INSPECTIONREPORT 05000458/2006003Dear Mr. Hinnenkamp:
SUBJECT:       RIVER BEND STATION - NRC INTEGRATED INSPECTION
On June 30, 2006, the U.S. Nuclear Regulatory Commission (NRC) completed an inspection atyour River Bend Station. The enclosed integrated inspection report documents the inspectionresults, which were discussed on July 5, 2006, with you and other members of your staff.The inspection examined activities conducted under your license as they relate to safety andcompliance with the Commission's rules and regulations and with the conditions of your license.  
                REPORT 05000458/2006003
Dear Mr. Hinnenkamp:
On June 30, 2006, the U.S. Nuclear Regulatory Commission (NRC) completed an inspection at
your River Bend Station. The enclosed integrated inspection report documents the inspection
results, which were discussed on July 5, 2006, with you and other members of your staff.
The inspection examined activities conducted under your license as they relate to safety and
compliance with the Commissions rules and regulations and with the conditions of your license.
The inspectors reviewed selected procedures and records, observed activities, and interviewed
The inspectors reviewed selected procedures and records, observed activities, and interviewed
personnel.The report documents three  
personnel.
NRC-identified findings and two self-revealing findings of very lowsafety significance (Green). The NRC has also determined that violations are associated withthese findings. However, because these violations were of very low safety significance and
The report documents three NRC-identified findings and two self-revealing findings of very low
safety significance (Green). The NRC has also determined that violations are associated with
these findings. However, because these violations were of very low safety significance and
were entered into your corrective action program, the NRC is treating these violations as
were entered into your corrective action program, the NRC is treating these violations as
noncited violations, consistent with Section VI.A.1 of the NRC Enforcement Policy. If youcontest the violations or the significance of the violations, you should provide a response within30 days of the date of this inspection report, with the basis for your denial, to the U.S. Nuclear
noncited violations, consistent with Section VI.A.1 of the NRC Enforcement Policy. If you
Regulatory Commission, ATTN: document Control Desk, Washington, DC 20555-0001, withcopies to the Regional Administrator, U.S. Nuclear Regulatory Commission, Region IV, 611
contest the violations or the significance of the violations, you should provide a response within
Ryan Plaza Drive, Suite 400, Arlington, Texas 76011-4005; the Director, Office of Enforcement,U.S. Nuclear Regulatory Commission, Washington, DC 20555-0001; and the NRC Resi dentInspector at the River Bend Station facility.In accordance with 10 CFR 2.390 of the NRC's "Rules of Practice," a copy of this letter, itsenclosure, and your response (if any) will be available electronically for public inspection in theNRC Public Document Room or from the Publicly Available Records (PARS) com
30 days of the date of this inspection report, with the basis for your denial, to the U.S. Nuclear
ponent ofNRC's document system (ADAMS). ADAMS is accessible from the NRC Website at
Regulatory Commission, ATTN: document Control Desk, Washington, DC 20555-0001, with
http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room).  
copies to the Regional Administrator, U.S. Nuclear Regulatory Commission, Region IV, 611
Entergy Operations, Inc.-2-Should you have any questions concerning this inspection, we will be pleased to discuss themwith you.Sincerely,/RA/Kriss M. Kennedy, ChiefProject Branch C
Ryan Plaza Drive, Suite 400, Arlington, Texas 76011-4005; the Director, Office of Enforcement,
Division of Reactor ProjectsDocket:   50-458License: NPF-47Enclosure:NRC Inspection Report 05000458/2006003  w/Attachment: Supplemental Informationcc w/enclosure:Senior Vice President and  
U.S. Nuclear Regulatory Commission, Washington, DC 20555-0001; and the NRC Resident
  Chief Operating Officer
Inspector at the River Bend Station facility.
In accordance with 10 CFR 2.390 of the NRCs Rules of Practice, a copy of this letter, its
enclosure, and your response (if any) will be available electronically for public inspection in the
NRC Public Document Room or from the Publicly Available Records (PARS) component of
NRCs document system (ADAMS). ADAMS is accessible from the NRC Website at
http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room).
 
Entergy Operations, Inc.                 -2-
Should you have any questions concerning this inspection, we will be pleased to discuss them
with you.
                                        Sincerely,
                                                /RA/
                                        Kriss M. Kennedy, Chief
                                        Project Branch C
                                        Division of Reactor Projects
Docket: 50-458
License: NPF-47
Enclosure:
NRC Inspection Report 05000458/2006003
   w/Attachment: Supplemental Information
cc w/enclosure:
Senior Vice President and
Chief Operating Officer
Entergy Operations, Inc.
Entergy Operations, Inc.
P.O. Box 31995
P.O. Box 31995
Jackson, MS 39286-1995Vice President Operations Support
Jackson, MS 39286-1995
Vice President
Operations Support
Entergy Operations, Inc.
Entergy Operations, Inc.
P.O. Box 31995
P.O. Box 31995
Jackson, MS 39286-1995General ManagerPlant Operations
Jackson, MS 39286-1995
General Manager
Plant Operations
Entergy Operations, Inc.
Entergy Operations, Inc.
River Bend Station
River Bend Station
5485 US Highway 61N
5485 US Highway 61N
St. Francisville, LA
St. Francisville, LA 70775
70775Director - Nuclear SafetyEntergy Operations, Inc.
Director - Nuclear Safety
Entergy Operations, Inc.
River Bend Station
River Bend Station
5485 US Highway 61N
5485 US Highway 61N
St. Francisville, LA
St. Francisville, LA 70775
70775Wise, Carter, Child & Caraway
Wise, Carter, Child & Caraway
P.O. Box 651
P.O. Box 651
Jackson, MS 39205  
Jackson, MS 39205
Entergy Operations, Inc.-3-Winston & Strawn LLP1700 K Street, N.W.
 
Washington, DC 20006-3817Manager - LicensingEntergy Operations, Inc.
Entergy Operations, Inc.             -3-
Winston & Strawn LLP
1700 K Street, N.W.
Washington, DC 20006-3817
Manager - Licensing
Entergy Operations, Inc.
River Bend Station
River Bend Station
5485 US Highway 61N
5485 US Highway 61N
St. Francisville, LA
St. Francisville, LA 70775
70775The Honorable Charles C. Foti, Jr.Attorney General
The Honorable Charles C. Foti, Jr.
Attorney General
Department of Justice
Department of Justice
State of Louisiana
State of Louisiana
P.O. Box 94005
P.O. Box 94005
Baton Rouge, LA 70804-9005H. Anne Plettinger
Baton Rouge, LA 70804-9005
3456 Villa Rose DriveBaton Rouge, LA 70806Bert Babers, PresidentWest Feliciana Parish Police Jury
H. Anne Plettinger
3456 Villa Rose Drive
Baton Rouge, LA 70806
Bert Babers, President
West Feliciana Parish Police Jury
P.O. Box 1921
P.O. Box 1921
St. Francisville, LA
St. Francisville, LA 70775
70775Richard Penrod, Senior Environmental   Scientist
Richard Penrod, Senior Environmental
Scientist
Office of Environmental Services
Office of Environmental Services
Northwestern State University  
Northwestern State University
Russell Hall, Room 201
Russell Hall, Room 201
Natchitoches, LA 71497Brian AlmonPublic Utility Commission
Natchitoches, LA 71497
Brian Almon
Public Utility Commission
William B. Travis Building
William B. Travis Building
P.O. Box 13326
P.O. Box 13326
1701 North Congress Avenue
1701 North Congress Avenue
Austin, TX 78711-3326  
Austin, TX 78711-3326
Entergy Operations, Inc.-4-ChairpersonDenton Field Office  
 
Chemical and Nuclear Preparedness  
Entergy Operations, Inc.           -4-
  and Protection Division
Chairperson
Denton Field Office
Chemical and Nuclear Preparedness
  and Protection Division
Office of Infrastructure Protection
Office of Infrastructure Protection
Preparedness Directorate
Preparedness Directorate
Line 83: Line 136:
800 North Loop 288
800 North Loop 288
Federal Regional Center
Federal Regional Center
Denton, TX 76201-3698  
Denton, TX 76201-3698
Entergy Operations, Inc.-5-Electronic distribution by RIV:Regional Administrator (BSM1)DRP Director (ATH)DRS Director (DDC)DRS Deputy Director (RJC1)Senior Resident Inspector (PJA)Branch Chief, DRP/C (KMK)Senior Project Engineer, DRP/C (WCW)Team Leader, DRP/TSS (RLN1)RITS Coordinator (KEG)DRS STA (DAP)J. Lamb, OEDO RIV Coordinator (JGL1)ROPreports
 
RBS Site Secretary (LGD)W. A. Maier, RSLO (WAM)SUNSI Review Completed: __wcw_     ADAMS:   Yes G No           Initials: __wcw___   Publicly Available       
Entergy Operations, Inc.                   -5-
G   Non-Publicly Available    
Electronic distribution by RIV:
G   Sensitive   Non-SensitiveR:\_REACTORS\_RB\2006\RB2006-03RP-PJA.wpdRIV:SRI:DRP/CRI:DRP/CC:DRS/OBC:DRS/EB1C:DRS/PSBPJAlterMOMillerATGodyJAClarkMPS
Regional Administrator (BSM1)
hannon T - WCWalker E - WCWalker   /RA/     /RA/     /RA/8/10/068/10/068/11/068/10/068/10/06C:DRS/EB2SRA:DRSC:DRP/CLJSmithDPLovelessKMKennedy    /RA/   /RA/     /RA/8/10/068/14/068/14/06OFFICIAL RECORD COPY T=Telephone           E=E-mail       F=Fax  
DRP Director (ATH)
Enclosure-1-U.S. NUCLEAR REGULATORY COMMISSIONREGION IVDocket:50-458License:NPF-47
DRS Director (DDC)
Report:05000458/2006003
DRS Deputy Director (RJC1)
Licensee:Entergy Operations, Inc.
Senior Resident Inspector (PJA)
Facility:River Bend StationLocation:5485 U.S. Highway 61St. Francisville, LouisianaDates:April 1 to June 30, 2006
Branch Chief, DRP/C (KMK)
Inspectors:P. Alter, Senior Resident Inspector, Project Branch CM. Miller, Resident Inspector, Project Branch CG. Werner, Senior Project Engineer, Project Branch D
Senior Project Engineer, DRP/C (WCW)
L. Ricketson, P.E., Senior Health Physicist, Plant Support Branch
Team Leader, DRP/TSS (RLN1)
W. Sifre, Senior Reactor Inspector, Engineering Branch 1Approved By:Kriss M. Kennedy, ChiefProject Branch C
RITS Coordinator (KEG)
Division of Reactor Projects  
DRS STA (DAP)
Enclosure-2-TABLE OF CONTENTSSUMMARY OF FINDINGS....................................................3REPORT DETAILS..........................................................6
J. Lamb, OEDO RIV Coordinator (JGL1)
REACTOR SAFETY.........................................................61R01Adverse Weather Protection
ROPreports
.......................................61R04Equipment Alignment
RBS Site Secretary (LGD)
.............................................71R05Fire Protection
W. A. Maier, RSLO (WAM)
..................................................71R08Inservice Inspection Activities
SUNSI Review Completed: __wcw_ ADAMS: : Yes G No                 Initials: __wcw___
......................................81R11Licensed Operator Requalification Program
: Publicly Available      G Non-Publicly Available G Sensitive   : Non-Sensitive
...........................91R12Maintenance Effectiveness.......................................101R13Maintenance Risk Assessments and Emergent Work Control.............101R14Operator Performance During Nonroutine Evolutions and Events..........111R15Operability Evaluations..........................................121R19Postmaintenance Testing........................................171R20Refueling and Other Outage Activities...............................171R22Surveillance Testing............................................201R23Temporary Plant Modifications....................................231EP6Drill Evaluation.................................................23RADIATION SAFETY.......................................................242OS1Access Control to Radiologically Significant Areas.....................242OS2ALARA Planning and Controls.....................................27OTHER ACTIVITIES........................................................284OA1Performance Indicator (PI) Verification..............................284OA2Identification and Resolution of Problems............................294OA3Event Followup................................................314OA5Other Activities.................................................324OA6Meetings, Including Exit..........................................32SUPPLEMENTAL INFORMATION............................................A-1
R:\_REACTORS\_RB\2006\RB2006-03RP-PJA.wpd
KEY POINTS OF CONTACT................................................A-1
RIV:SRI:DRP/C          RI:DRP/C        C:DRS/OB      C:DRS/EB1        C:DRS/PSB
LIST OF ITEMS OPENED, CLOSED, AND DISCUSSED...........................A-1LIST OF DOCUMENTS REVIEWED..........................................A-2
  PJAlter                MOMiller        ATGody        JAClark          MPShannon
LIST OF ACRONYMS......................................................A-7  
  T - WCWalker         E - WCWalker     /RA/           /RA/             /RA/
Enclosure-3-SUMMARY OF FINDINGSIR 05000458/2006003; 04/01/2006 - 06/30/2006; River Bend Station; Operability Evaluations,Refueling and Other Outage Activities, Surveillance Testing, Occupational Radiation Safety.The report covered a 3-month period of routine baseline inspections by resident inspectors andannounced baseline inspections by regional engineering and radiation protection inspectors.  
8/10/06                8/10/06        8/11/06        8/10/06          8/10/06
Five Green noncited violations were identified. The significance of most findings is indicated by
C:DRS/EB2              SRA:DRS        C:DRP/C
their color (Green, White, Yellow, Red) using Inspection Manual Chapter 0609, "Significance
LJSmith                DPLoveless      KMKennedy
Determination Process.Findings for which the significance determination process does not
    /RA/                   /RA/             /RA/
apply may be Green or be assigned a severity level after  
8/10/06                8/14/06        8/14/06
NRC management review. TheNRC's program for overseeing the safe operation of commercial nuclear power reactors isdescribed in NUREG-1649, "Reactor Oversight Process," Revision 3, dated July 2000.A.NRC-Identified and Self-Revealing FindingsCornerstone: Mitigating SystemsGreen. A self-revealing noncited violation of 10 CFR Part 50, Appendix B, Criterion XVI,"Corrective Action," was reviewed involving the failure of the licensee to identify that the
OFFICIAL RECORD COPY                               T=Telephone     E=E-mail     F=Fax
normal supply breaker to the Division III 4.16 kV engineered safety features bus was notproperly racked in for a period of 24 days following maintenance. This issue was
 
entered into the licensee's corrective action program as CR-RBS-2006-02402.The finding was more than minor because it was associated with the mitigating systemcornerstone attribute of configuration control and affected the associated cornerstone
              U.S. NUCLEAR REGULATORY COMMISSION
objective to ensure the availability, reliability, and capability of systems that res
                                  REGION IV
pond toinitiating events to prevent undesirable consequences. Utilizing Manual Chapter 0609,"Significance Determination Process," a Phase 3 analysis concluded that the finding
Docket:     50-458
was of very low safety significance. The cause of the finding was related to the
License:     NPF-47
crosscutting aspect of problem identification and resolution in that the licensee failed toproperly evaluate available indications to identify that the breaker was not properly
Report:     05000458/2006003
racked in. (Section 1R15).Green. An NRC identified noncited violation of 10 CFR 50.65 Maintenance RuleSection (a)(4) was identified for the failure of the licensee to provide prescribed
Licensee:   Entergy Operations, Inc.
compensatory measures for two Orange shutdown risk conditions during Refueling
Facility:   River Bend Station
Outage 13. Specifically, the preoutage risk assessment recommended that two workorders be in place for maintenance electricians to provide power to one spent fuel pool
Location:   5485 U.S. Highway 61
cooling pump in the event of problems with the running pump during periods of electrical
            St. Francisville, Louisiana
bus maintenance. The inspectors found that the work packages were not in place
Dates:       April 1 to June 30, 2006
before entering shutdown risk condition Orange on April 26, 2006, during the Division II
Inspectors: P. Alter, Senior Resident Inspector, Project Branch C
engineering safety features bus testing, and May 3, 2006, during the Division I
            M. Miller, Resident Inspector, Project Branch C
engineered safety features bus outage. This issue was entered into the licensee's
            G. Werner, Senior Project Engineer, Project Branch D
corrective action program as CR-RBS-2006-01937.The finding was more than minor because the licensee failed to implement a prescribedcompensatory measure during the highest risk condition of Refueling Outage 13. The  
            L. Ricketson, P.E., Senior Health Physicist, Plant Support Branch
Enclosure-4-specific compensatory measures were called for in the preoutage risk assessment andthe shutdown operations protection plan. The finding affected the mitigati ng syst emcornerstone because of the increased risk of a sustained loss of spent fuel pool cooling
            W. Sifre, Senior Reactor Inspector, Engineering Branch 1
during core offloading operations. The finding could not be evaluated using the
Approved By: Kriss M. Kennedy, Chief
significance determination process, therefore the finding was reviewed by regional
            Project Branch C
management and determined to be of very low safety significance. Factors that were
            Division of Reactor Projects
considered included: (1) electrical maintenance technicians had previously performed
                                      -1-                                 Enclosure
the task of providing alternate power to a spent fuel pool cooling pump, (2) the
 
necessary equipment was staged as part of the abnormal operating procedure for loss
                                      TABLE OF CONTENTS
of decay heat removal, and (3) the relatively long "time to boil" of the spent fuel storage
SUMMARY OF FINDINGS . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 3
pool at that time during the refueling outage. The cause of the finding was related to thecrosscutting aspect of human performance because the licensee's plannedmaintenance activities and the predetermined increase in outage risk was not effectively
REPORT DETAILS . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 6
managed by prescribed compensatory measures (Section 1R20).Green. An NRC identified noncited violation of Technical Specification 5.4.1.a wasidentified for the failure of the licensee to provide an adequate surveillance testprocedure to perform Technical Specification Surveillance Requirement 3.8.1.1. Specifically, STP-000-0102, "Power Distribution Alignment Check," Revision 4, did not
REACTOR SAFETY . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 6
verify the required offsite power circuit breaker alignment and indicated power
      1R01 Adverse Weather Protection . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 6
availability for the Division III 4.16 kV engineered safety features bus as required inModes 1, 2, and 3. This issue was entered into the licensee's corrective action program
      1R04 Equipment Alignment . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 7
as CR-RBS-2006-02675 and -02402.The finding was more than minor because it was associated with the mitigating systemcornerstone attribute of configuration control and affected the associated cornerstone
      1R05 Fire Protection . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 7
objective to ensure the availability, reliability, and capability of systems that res
      1R08 Inservice Inspection Activities . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 8
pond toinitiating events to prevent undesirable consequences. Utilizing Manual Chapter 0609,"Significance Determination Process," a Phase 3 analysis concluded that the finding
      1R11 Licensed Operator Requalification Program . . . . . . . . . . . . . . . . . . . . . . . . . . . 9
was of very low safety significance. (Section 1R22).Cornerstone: Occupational Radiation Safety
      1R12 Maintenance Effectiveness . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 10
*Green. The inspector reviewed a self-revealing noncited violation of TechnicalSpecification 5.7.1, resulting from the licensee's failure to control access to a high
      1R13 Maintenance Risk Assessments and Emergent Work Control . . . . . . . . . . . . . 10
radiation area. While transferring reverse osmosis system filters in the radwaste
      1R14 Operator Performance During Nonroutine Evolutions and Events . . . . . . . . . . 11
building, the licensee allowed two workers to inadvertently enter a high radiation area. This occurred after a guard prematurely left his post in front of the 123 foot elevation
      1R15 Operability Evaluations . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 12
elevator door. The highest dose rate recorded by an electronic alarming dosimeter was
      1R19 Postmaintenance Testing . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 17
164 millirem per hour. The guard returned and evacuated the workers before they accrued additional radiation dose. Planned corrective action was still being evaluated bythe licensee at the conclusion of the inspection.The finding was more than minor because it was associated with the occupationalradiation safety attribute of exposure control and affected the cornerstone objective in
      1R20 Refueling and Other Outage Activities . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 17
that not controlling a high radiation area could increase personal exposure. Using theOccupational Radiation Safety Significance Determination Process, the inspector
      1R22 Surveillance Testing . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 20
determined that the finding was of very low safety significance because it did not  
      1R23 Temporary Plant Modifications . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 23
Enclosure-5-involve: (1) an as low as is reasonably achievable finding, (2) an overexposure, (3) asubstantial potential for overexposure, or (4) an impaired ability to assess dose.  
      1EP6 Drill Evaluation . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 23
Additionally, this finding had crosscutting aspects associated with human performancein that the failure of the individual to guard the elevator door directly contributed to theviolation. (Section 2OS1)*Green. The inspector identified a noncited violation of 10 CFR 20.1501(a) because thelicense failed to survey airborne radioactivity. During the removal of local power range
RADIATION SAFETY . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 24
monitors, the licensee started collecting an air sample of the work area, but discarded
      2OS1 Access Control to Radiologically Significant Areas . . . . . . . . . . . . . . . . . . . . . 24
the sample before analyzing it. Successful passage through the portal monitors at the
      2OS2 ALARA Planning and Controls . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 27
exit of the controlled access area confirmed that no worker experienced an uptake of
OTHER ACTIVITIES . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 28
radioactive material. Planned corrective action is still being evaluated.The finding was more than minor because it was associated with the occupationalradiation safety program attribute of exposure control and affected the cornerstone
      4OA1 Performance Indicator (PI) Verification . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 28
objective in that the lack of knowledge of radiological conditions could increase
      4OA2 Identification and Resolution of Problems . . . . . . . . . . . . . . . . . . . . . . . . . . . . 29
personnel dose. Using the Occupational Radiation Safety Significance Determination
      4OA3 Event Followup . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 31
Process, the inspector determined that the finding was of very low safety significance
      4OA5 Other Activities . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 32
because it did not involve: (1) an as low as is reasonably achievable finding, (2) an
      4OA6 Meetings, Including Exit . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 32
overexposure, (3) a substantial potential for overexposure, or (4) an impaired ability to
SUPPLEMENTAL INFORMATION . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . A-1
assess dose. Additionally, this finding had crosscutti
KEY POINTS OF CONTACT . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . A-1
ng aspects associated with humanperformance in that the failure to maintain the sample for analysis directly contributed to
LIST OF ITEMS OPENED, CLOSED, AND DISCUSSED . . . . . . . . . . . . . . . . . . . . . . . . . . . A-1
the violation.  (Section 2OS1)B.Licensee-Identified ViolationsNone.
LIST OF DOCUMENTS REVIEWED . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . A-2
Enclosure-6-REPORT DETAILSSummary of Plant Status:  The reactor was operated at 100 percent power from April 1-15,2006, when the reactor scrammed due to a control circuit failure which caused both reactor
LIST OF ACRONYMS . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . A-7
recirculation pumps to shift to slow speed. The reactor was restarted on April 17 and attained
                                                        -2-                                                         Enclosure
100 percent power on April 18. On April 23, the reactor was shut down for Refueling Outage
 
(RFO) -13. On May 12, the reactor was restarted and attained 100 percent power on May 18.  
                                    SUMMARY OF FINDINGS
IR 05000458/2006003; 04/01/2006 - 06/30/2006; River Bend Station; Operability Evaluations,
Refueling and Other Outage Activities, Surveillance Testing, Occupational Radiation Safety.
The report covered a 3-month period of routine baseline inspections by resident inspectors and
announced baseline inspections by regional engineering and radiation protection inspectors.
Five Green noncited violations were identified. The significance of most findings is indicated by
their color (Green, White, Yellow, Red) using Inspection Manual Chapter 0609, Significance
Determination Process. Findings for which the significance determination process does not
apply may be Green or be assigned a severity level after NRC management review. The
NRCs program for overseeing the safe operation of commercial nuclear power reactors is
described in NUREG-1649, Reactor Oversight Process, Revision 3, dated July 2000.
A.     NRC-Identified and Self-Revealing Findings
Cornerstone: Mitigating Systems
        Green. A self-revealing noncited violation of 10 CFR Part 50, Appendix B, Criterion XVI,
        "Corrective Action," was reviewed involving the failure of the licensee to identify that the
        normal supply breaker to the Division III 4.16 kV engineered safety features bus was not
        properly racked in for a period of 24 days following maintenance. This issue was
        entered into the licensee's corrective action program as CR-RBS-2006-02402.
        The finding was more than minor because it was associated with the mitigating system
        cornerstone attribute of configuration control and affected the associated cornerstone
        objective to ensure the availability, reliability, and capability of systems that respond to
        initiating events to prevent undesirable consequences. Utilizing Manual Chapter 0609,
        "Significance Determination Process," a Phase 3 analysis concluded that the finding
        was of very low safety significance. The cause of the finding was related to the
        crosscutting aspect of problem identification and resolution in that the licensee failed to
        properly evaluate available indications to identify that the breaker was not properly
        racked in. (Section 1R15).
        Green. An NRC identified noncited violation of 10 CFR 50.65 Maintenance Rule
        Section (a)(4) was identified for the failure of the licensee to provide prescribed
        compensatory measures for two Orange shutdown risk conditions during Refueling
        Outage 13. Specifically, the preoutage risk assessment recommended that two work
        orders be in place for maintenance electricians to provide power to one spent fuel pool
        cooling pump in the event of problems with the running pump during periods of electrical
        bus maintenance. The inspectors found that the work packages were not in place
        before entering shutdown risk condition Orange on April 26, 2006, during the Division II
        engineering safety features bus testing, and May 3, 2006, during the Division I
        engineered safety features bus outage. This issue was entered into the licensee's
        corrective action program as CR-RBS-2006-01937.
        The finding was more than minor because the licensee failed to implement a prescribed
        compensatory measure during the highest risk condition of Refueling Outage 13. The
                                                  -3-                                     Enclosure
 
      specific compensatory measures were called for in the preoutage risk assessment and
      the shutdown operations protection plan. The finding affected the mitigating system
      cornerstone because of the increased risk of a sustained loss of spent fuel pool cooling
      during core offloading operations. The finding could not be evaluated using the
      significance determination process, therefore the finding was reviewed by regional
      management and determined to be of very low safety significance. Factors that were
      considered included: (1) electrical maintenance technicians had previously performed
      the task of providing alternate power to a spent fuel pool cooling pump, (2) the
      necessary equipment was staged as part of the abnormal operating procedure for loss
      of decay heat removal, and (3) the relatively long time to boil of the spent fuel storage
      pool at that time during the refueling outage. The cause of the finding was related to the
      crosscutting aspect of human performance because the licensees planned
      maintenance activities and the predetermined increase in outage risk was not effectively
      managed by prescribed compensatory measures (Section 1R20).
      Green. An NRC identified noncited violation of Technical Specification 5.4.1.a was
      identified for the failure of the licensee to provide an adequate surveillance test
      procedure to perform Technical Specification Surveillance Requirement 3.8.1.1.
      Specifically, STP-000-0102, Power Distribution Alignment Check, Revision 4, did not
      verify the required offsite power circuit breaker alignment and indicated power
      availability for the Division III 4.16 kV engineered safety features bus as required in
      Modes 1, 2, and 3. This issue was entered into the licensee's corrective action program
      as CR-RBS-2006-02675 and -02402.
      The finding was more than minor because it was associated with the mitigating system
      cornerstone attribute of configuration control and affected the associated cornerstone
      objective to ensure the availability, reliability, and capability of systems that respond to
      initiating events to prevent undesirable consequences. Utilizing Manual Chapter 0609,
      "Significance Determination Process," a Phase 3 analysis concluded that the finding
      was of very low safety significance. (Section 1R22).
Cornerstone: Occupational Radiation Safety
*     Green. The inspector reviewed a self-revealing noncited violation of Technical
      Specification 5.7.1, resulting from the licensees failure to control access to a high
      radiation area. While transferring reverse osmosis system filters in the radwaste
      building, the licensee allowed two workers to inadvertently enter a high radiation area.
      This occurred after a guard prematurely left his post in front of the 123 foot elevation
      elevator door. The highest dose rate recorded by an electronic alarming dosimeter was
      164 millirem per hour. The guard returned and evacuated the workers before they
      accrued additional radiation dose. Planned corrective action was still being evaluated by
      the licensee at the conclusion of the inspection.
      The finding was more than minor because it was associated with the occupational
      radiation safety attribute of exposure control and affected the cornerstone objective in
      that not controlling a high radiation area could increase personal exposure. Using the
      Occupational Radiation Safety Significance Determination Process, the inspector
      determined that the finding was of very low safety significance because it did not
                                                -4-                                     Enclosure
 
  involve: (1) an as low as is reasonably achievable finding, (2) an overexposure, (3) a
  substantial potential for overexposure, or (4) an impaired ability to assess dose.
  Additionally, this finding had crosscutting aspects associated with human performance
  in that the failure of the individual to guard the elevator door directly contributed to the
  violation. (Section 2OS1)
* Green. The inspector identified a noncited violation of 10 CFR 20.1501(a) because the
  license failed to survey airborne radioactivity. During the removal of local power range
  monitors, the licensee started collecting an air sample of the work area, but discarded
  the sample before analyzing it. Successful passage through the portal monitors at the
  exit of the controlled access area confirmed that no worker experienced an uptake of
  radioactive material. Planned corrective action is still being evaluated.
  The finding was more than minor because it was associated with the occupational
  radiation safety program attribute of exposure control and affected the cornerstone
  objective in that the lack of knowledge of radiological conditions could increase
  personnel dose. Using the Occupational Radiation Safety Significance Determination
  Process, the inspector determined that the finding was of very low safety significance
  because it did not involve: (1) an as low as is reasonably achievable finding, (2) an
  overexposure, (3) a substantial potential for overexposure, or (4) an impaired ability to
  assess dose. Additionally, this finding had crosscutting aspects associated with human
  performance in that the failure to maintain the sample for analysis directly contributed to
  the violation. (Section 2OS1)
B. Licensee-Identified Violations
  None.
                                              -5-                                      Enclosure
 
                                      REPORT DETAILS
Summary of Plant Status: The reactor was operated at 100 percent power from April 1-15,
2006, when the reactor scrammed due to a control circuit failure which caused both reactor
recirculation pumps to shift to slow speed. The reactor was restarted on April 17 and attained
100 percent power on April 18. On April 23, the reactor was shut down for Refueling Outage
(RFO) -13. On May 12, the reactor was restarted and attained 100 percent power on May 18.
On June 15, reactor power was reduced to 23 percent because of a problem with the main
On June 15, reactor power was reduced to 23 percent because of a problem with the main
turbine bypass valves. The reactor was returned to 100 percent power on June 18. The
turbine bypass valves. The reactor was returned to 100 percent power on June 18. The
reactor remained at 100 percent power for the remainder of the inspection period, with the
reactor remained at 100 percent power for the remainder of the inspection period, with the
exception of regularly scheduled power reductions for control rod pattern adjustments and
exception of regularly scheduled power reductions for control rod pattern adjustments and
turbine testing.1.REACTOR SAFETYCornerstones: Initiating Events, Mitigating Systems, Barrier Integrity, EmergencyPreparedness1R01Adverse Weather Protection     a.Inspection ScopeHurricane Season PreparationsDuring the week of June 12, 2006, the inspectors completed a review of the licensee'sreadiness for seasonal susceptibilities involving high winds at the beginning of hurricaneseason. The inspectors reviewed Procedure ENS-EP-302, "Severe Weather
turbine testing.
Response," Revision 4. The inspectors: (1) reviewed plant procedures, the Updated
1.     REACTOR SAFETY
Safety Analysis Report (USAR), and Technical Specifications (TS) to verify that operator
        Cornerstones: Initiating Events, Mitigating Systems, Barrier Integrity, Emergency
actions defined in adverse weather procedures maintained the readiness of essential
        Preparedness
systems; (2) walked down portions of the protected area to verify that hurri
1R01 Adverse Weather Protection
cane seasonpreparations were sufficient to support operability of essential systems, including theability to perform safe shutdown functions; (3) evaluated operator staffing levels to verifythe licensee could maintain the readiness of essential systems required by plantprocedures; and (4) reviewed the corrective action program (CAP) to determine if the
  a.   Inspection Scope
licensee identified and corrected problems related to adverse weather conditions.The inspectors completed one inspection sample.    b.FindingsNo findings of significance were identified.
        Hurricane Season Preparations
Enclosure-7-1R04Equipment Alignment  Partial System Walkdowns    a.Inspection ScopeThe inspectors:  (1) walked down portions of the three risk important systems listedbelow and review
        During the week of June 12, 2006, the inspectors completed a review of the licensee's
ed system operating procedures (SOPs), piping and instrumentdiagrams, and other documents to verify that critical portions of the selected systemswere correctly aligned; and (2) compared deficiencies identified during the walkdown to
        readiness for seasonal susceptibilities involving high winds at the beginning of hurricane
the licensee's USAR and CAP to verify problems were being identified and corrected. *Alternate decay heat removal system, which was the backup to the inserviceshutdown cooling system during refueling operations, on May 2, 2006*Reactor core isolation cooling system, while the high pressure core spray dieselwas out of service for maintenance, on June 12, 2006*Division I emergency diesel generator (EDG), while Division II EDG was out ofservice for planned maintenance, on June 21, 2006 Documents reviewed by the inspectors included:
        season. The inspectors reviewed Procedure ENS-EP-302, Severe Weather
*SOP-0140, "Suppression Pool Cleanup and Alternate Decay Heat Removal,"Revision 16*SOP-0035, "Reactor Core Isolation Cooling System," Revision 8A
        Response, Revision 4. The inspectors: (1) reviewed plant procedures, the Updated
*SOP-0053, "Standby Diesel Generator and Auxiliaries," Revision 44AThe inspectors completed three inspection samples.    h.FindingsNo findings of significance were identified.1R05Fire Protection    b.Inspection ScopeThe inspectors walked down the six plant areas listed below to assess the materialcondition of active and passive fire protection features and their operational lineup and
        Safety Analysis Report (USAR), and Technical Specifications (TS) to verify that operator
readiness.  The inspectors:  (1) verified that transient combustibles were controlled in
        actions defined in adverse weather procedures maintained the readiness of essential
accordance with plant procedures; (2) observed the condition of fire detection devices to
        systems; (2) walked down portions of the protected area to verify that hurricane season
verify they remained functional; (3) observed fire suppression systems to verify theyremained functional and that access to manual actuators was unobstructed; (4) verified
        preparations were sufficient to support operability of essential systems, including the
that fire extinguishers and hose stations were provided at their designated locations and
        ability to perform safe shutdown functions; (3) evaluated operator staffing levels to verify
Enclosure-8-that they were in a satisfactory condition; (5) verified that passive fire protection features(electrical raceway barriers, fire doors, fire dampers, steel fire proofing, penetration
        the licensee could maintain the readiness of essential systems required by plant
seals, and oil collection systems) were in a satisfactory material condition; (6) verifiedthat adequate compensatory measures were established for degraded or inoperable fire
        procedures; and (4) reviewed the corrective action program (CAP) to determine if the
protection features and that the compensatory measures were commensurate with thesignificance of the deficiency; and (7) reviewed the CAP to determine if the licensee
        licensee identified and corrected problems related to adverse weather conditions.
identified and corrected fire protection problems. *Auxiliary building piping Tunnel D, Fire Area AB-7, on May 9, 2006*Low pressure core spray pump room, Fire Area AB-6/Z-1, on May 9, 2006
        The inspectors completed one inspection sample.
*High pressure core spray pump room, Fire Area AB-2/Z-1, on May 9, 2006
  b.   Findings
*Control building standby switchgear Room 1A, Fire Area C-15, on June 22, 2006
        No findings of significance were identified.
*Control building safety related cable tray area and stairway Number 3, Fire AreaC-16 and C-29, on June 22, 2006*Division I EDG control and diesel engine rooms, Fire Area DG-6/Z-1, on June 22, 2006Documents reviewed by the inspectors included:
                                                -6-                                     Enclosure
*Pre-Fire Plan/Strategy Book*USAR Section 9A.2, "Fire Hazards Analysis," Revision 10
*River Bend Station postfire safe shutdown analysis
*RBNP-038, "Site Fire Protection Program," Revision 6BThe inspectors completed six inspection samples.    b.FindingsNo findings of significance were identified.1R08Inservice Inspection Activities    a.Inspection ScopeThe inspector witnessed the performance of 12 volumetric (ultrasonic) and four surface(liquid penetrant) examinations.  The sample of nondestructive examination (NDE)
activities is listed in the attachment. For each of the NDE activities reviewed, the inspector verified that the examinationswere performed in accordance with American Society of Mechanical Engineers (ASME)
Code requirements.
Enclosure-9-During the review of each examination, the inspector verified that appropriate NDEprocedures were used, that examinations and conditions were as specified in the
procedure, and that test instrumentation or equipment was properly calibrated and withinthe allowable calibration period.  The inspector also reviewed documentation to verify
that indications revealed by the examinations were  dispositioned in accordance with the
ASME Code specified acceptance standards.  The inspector verified the certifications of the NDE personnel observed performingexaminations or identified during review of completed examination packages.The inspection procedure requires review of one or two examinations from the previousoutage with recordable indications that were accepted for continued service to ensure
that the disposition was done in accordance with the ASME Code.  There were no
recordable indications that required evaluation during the last outage.  If the licensee completed welding on the pressure boundary for Class 1 or
2 systemssince the beginning of the previous outage, the procedure requires verification thatacceptance and preservice examinations were done in accordance with the ASME Code
for one to three welds.  There were no welds available for review.The procedure also requires verification that one or two ASME Code Section XI repairsor replacements meet code requirements.  There were no code repairs or replacements
available at the time of this inspection.The inspectors completed 16 inspection samples.    b.FindingsNo findings of significance were identified.1R11Licensed Operator Requalification Program    a.Inspection ScopeOn June 13, 2006, the inspectors observed testing and training of senior reactoroperators and reactor operators to verify the adequacy of training, to assess operator
performance, and to assess the evaluators' critique.  The training evaluation scenario
observed was RSMS-OPS-422, "Loss of Circ Water Pump, Failure of Steam Flow
Transmitter and Instrument Air System Leak," Revision 4.The inspectors completed one inspection sample.    b.FindingsNo findings of significance were identified.  
Enclosure-10-1R12Maintenance Effectiveness    a.Inspection ScopeThe inspectors reviewed the condition reports (CR) listed below which documentedequipment problems to:  (1) verify the appropriate handling of structure, system , andcomponent (SSC) performance or condition problems; (2) verify the appropriate
handling of degraded SSC functional performance; (3) evaluate the role of work
practices and common cause problems; and (4) evaluate the handling of SSC issues
reviewed under the requirements of the maintenance rule; 10 CFR Part 50, Appendix B;
and TS. *CR-RBS-2006-1898, main steam stop Valve B21-MOVF098C leakage, reviewedon June 2, 2006, and CR-RBS-2004-4338, main steam stop Valve B21-
MOVF098C high leakage during RFO-11 and -12, reviewed on June 26, 2006.*CR-RBS-2006-2302, primary containment integrity maintenance rule repetitivefunctional failure, reviewed on June 26, 2006.Documents reviewed by the inspectors included:
*NUMARC 93-01, Nuclear Energy Institute Industry (NEI) Guideline for Monitoringthe Effectiveness of Maintenance at Nuclear Power Plants, Revision 2*Maintenance rule function list
*Maintenance rule performance criteria list
*Main steam stop valve maintenance rule performance evaluations
The inspectors completed two inspection samples.    b.FindingsNo findings of significance were identified.1R13Maintenance Risk Assessments and Emergent Work Control    a.Inspection Scope    .1Risk Assessment and Management of RiskThe inspectors reviewed the planned work weeks listed below to verify:  (1) that thelicensee performed risk assessments when required by 10 CFR 50.65 (a)(4) and
administrative Procedure ADM-096, "Risk Management Program Implementation and
On-Line Maintenance Risk Assessment," Revision 4B, prior to changes in plant
configuration for maintenance activities and plant operations; (2) the accuracy,
adequacy, and completeness of the information considered in the risk assessment;
Enclosure-11-(3) that the licensee recognized, and entered as applicable, the appropriate licenseeestablished risk category according to the risk assessment results and Procedure ADM-
096; and (4) that the licensee identified and corrected problems related to maintenancerisk assessments.  Specific work activities evaluated included planned and emergent
work for the weeks of:*June 5, 2006, Division I work week and preferred station service TransformerRTX-ESR1F cooling oil dehydration*June 19, 2006, planned Division II EDG outage week
*June 26, 2006, nondivisional work week and potential labor work stoppage    .2Emergent Work ControlFor the two emergent work activities listed below, the inspectors:  (1) verified that thelicensee performed actions to minimize the probability of initiating events andmaintained the functional capability of mitigating systems and barrier integrity systems;(2) verified that emergent work related activities such as troubleshooting, work
planning/scheduling, establishing plant conditions, aligning equipment, tagging,
temporary modifications, and equipment restoration did not place the plant in an
unacceptable configuration; and (3) reviewed the CAP to determine if the licenseeidentified and corrected risk assessment and emergent work control problems. *Preferred station service Transformer RTX-ESR1F sudden pressure relay failureon May 30, 2006*Main turbine bypass valves inoperable due to hydraulic oil leak on June 2, 2006
The inspectors completed five inspection samples.    c.FindingsNo findings of significance were identified.1R14Operator Performance During Nonroutine Evolutions and Events    a.Inspection Scope    1.April 4, 2006, Automatic Initiation of Standby Service WaterThe inspectors:  (1) reviewed operator logs, plant computer data, and strip charts for theApril 4, 2006, unexpected initiation of Division II standby service water that occurred
while swapping the running normal service water pumps to evaluate operator
performance in coping with the event; (2) verified that operator actions were in
accordance with the response required by plant procedures and training; and (3) verified
that the licensee identified and implemented appropriate corrective actions associatedwith personnel performance problems that occurred during the transient.  In addition, the
Enclosure-12-inspectors reviewed CR-RBS-2006-01257, which documented the procedural problemsthat led to the event and reviewed the following procedures used by the operators:*AOP-53, "Initiation of Standby Service Water With Normal Service WaterRunning," Revision 8*SOP-42, "Standby Service Water System," Revision 25
*SOP-66, "Control Building HVAC Chilled Water System," Revision 33B    2.April 15, 2006, Reactor ScramThe inspectors:  (1) reviewed operator logs, plant computer data, and strip charts for theApril 15, 2006, unexpected reactor recirculation pump downshift and subsequent reactor
scram to evaluate operator performance in coping with the event; (2) verified that
operator actions were in accordance with the response required by plant procedures
and training; and (3) verified that the licensee identified and implemented appropriatecorrective actions associated with personnel performance problems that occurred during
the transient.  In addition the inspectors reviewed the postscram report documented in
Procedure GOP-003, "Scram Recovery," Revision 16A, and observed the onsite safety
review committee review of the postscram report.The inspectors completed two inspection samples.    e.FindingsNo findings of significance were identified.1R15Operability Evaluations    a.Inspection ScopeFor the operability evaluations associated with the documents listed below, theinspectors:  (1) reviewed plants status documents such as operator shift logs, emergent
work documentation, deferred modifications, and standing orders, to determine if an
operability evaluation was warranted for degraded components; (2) referred to theUSAR and design basis documents to review the technical adequacy of licensee
operability evaluations; (3) evaluated compensatory measures associated withoperability evaluations; (4) determined degraded component impact on any TS; (5) usedthe significance determination process to evaluate the risk significance of degraded or
inoperable equipment; and (6) verified that the licensee identified and implemented
appropriate corrective actions associated with degraded components. *CR-RBS-2006-01207 and -01215, Primary containment purge exhaust line failsto meet leak rate acceptance criteria, reviewed during the week of April 3, 2006
Enclosure-13-*CR-RBS-2005-02805, Inserted control Rod 24-29 control blade lifetimecalculation revised for extended operating cycle, reviewed during the week ofApril 17, 2006*Work Request (WR) 76625, NNS-ACB23 "control power" light out, suspect badsocket, reviewed during the week of May 29, 2006*TS-LCO-06-0711, Division II EDG Generator Output Breaker charging springsdid not charge during tagout restoration, reviewed on June 23, 2006*CR-RBS-2006-01257, Division II standby service water start on low service waterpressure, reviewed on June 28, 2006*CR-RBS-2006-02632, turbine bypass valves hydraulic oil leak, reviewed onJune 28, 2006Other documents reviewed by the inspectors are listed in the attachment.
The inspectors completed six inspection samples.    b.FindingsIntroduction:  The inspectors reviewed a self-revealing noncited violation (NCV) of10 CFR Part 50, Appendix B, Criterion XVI, "Corrective Action," involving the failure of
the licensee to identify that the normal supply breaker to the Division III 4.16 kVengineered safety features (ESF) bus was not properly racked in following maintenance. Description:  Following the completion of planned maintenance on Switchgear NNS-SWG1A on April 29, 2006, operators were assigned to clear equipment tags and restore


the system alignment. As part of this task, operators racked in Breaker NNS-ACB23,the normal supply breaker to 4.16 kV Switchgear NNS-SWG1C. No actions, such as
1R04 Equipment Alignment
cycling the breaker, were required to verify that the breaker was properly racked in.On May 9, 2006, after noting that the control power light associated with Breaker NNS-ACB23 was not lit, operators wrote WR 76625 to repair the light. The WR stated that
Partial System Walkdowns
the white control power light on Control Room Panel H13-P808 was out with the breakerracked in and the control power fuses installed. The WR also indicated that the
  a.  Inspection Scope
suspected cause was a bad socket and that position Switch 52H had failed in the past to
      The inspectors: (1) walked down portions of the three risk important systems listed
make up during closure. A work control center senior reactor operator determined that
      below and reviewed system operating procedures (SOPs), piping and instrument
an operability evaluation was not required for the condition described in WR 76625. TheWR was classified "4D," which indicated that it should be scheduled as resources
      diagrams, and other documents to verify that critical portions of the selected systems
allowed within the normal 16-week work planning schedule. The inspectors noted the
      were correctly aligned; and (2) compared deficiencies identified during the walkdown to
licensee did not write a CR. The white control power light provides indication that the
      the licensee's USAR and CAP to verify problems were being identified and corrected.
breaker is functional, specifically, that: (1) there is no electrical fault on the line or load
      *        Alternate decay heat removal system, which was the backup to the inservice
side of the breaker, (2) the breaker "Lockout" button is not depressed on Panel 808, and(3) the breaker is fully racked into the switchgear. On May 9, 2006, there were no
                shutdown cooling system during refueling operations, on May 2, 2006
electrical faults on Breaker NNS-ACB23 and the "Lockout" was reset on Panel 808.
      *        Reactor core isolation cooling system, while the high pressure core spray diesel
Enclosure-14-On May 22, 2006, while aligning Switchgear NNS-SWG1C and the Division III 4.16 kVESF bus to the Transformer RSS1 offsite power supply, Breaker NNS-ACB23 failed to
                was out of service for maintenance, on June 12, 2006
close. Operators racked the breaker out and in, but the breaker failed to close on thesecond attempt. Subsequent troubleshooting identified that the breaker had not beenfully racked in as electricians were able to rotate the racking device one additional turn.  
      *        Division I emergency diesel generator (EDG), while Division II EDG was out of
The white light on Panel 808 came on and the breaker was successfully closed. The
                service for planned maintenance, on June 21, 2006
      Documents reviewed by the inspectors included:
      *        SOP-0140, Suppression Pool Cleanup and Alternate Decay Heat Removal,
                Revision 16
      *        SOP-0035, Reactor Core Isolation Cooling System, Revision 8A
      *        SOP-0053, Standby Diesel Generator and Auxiliaries, Revision 44A
      The inspectors completed three inspection samples.
  h.  Findings
      No findings of significance were identified.
1R05 Fire Protection
  b.  Inspection Scope
      The inspectors walked down the six plant areas listed below to assess the material
      condition of active and passive fire protection features and their operational lineup and
      readiness. The inspectors: (1) verified that transient combustibles were controlled in
      accordance with plant procedures; (2) observed the condition of fire detection devices to
      verify they remained functional; (3) observed fire suppression systems to verify they
      remained functional and that access to manual actuators was unobstructed; (4) verified
      that fire extinguishers and hose stations were provided at their designated locations and
                                                -7-                                      Enclosure
 
    that they were in a satisfactory condition; (5) verified that passive fire protection features
    (electrical raceway barriers, fire doors, fire dampers, steel fire proofing, penetration
    seals, and oil collection systems) were in a satisfactory material condition; (6) verified
    that adequate compensatory measures were established for degraded or inoperable fire
    protection features and that the compensatory measures were commensurate with the
    significance of the deficiency; and (7) reviewed the CAP to determine if the licensee
    identified and corrected fire protection problems.
    *        Auxiliary building piping Tunnel D, Fire Area AB-7, on May 9, 2006
    *        Low pressure core spray pump room, Fire Area AB-6/Z-1, on May 9, 2006
    *        High pressure core spray pump room, Fire Area AB-2/Z-1, on May 9, 2006
    *        Control building standby switchgear Room 1A, Fire Area C-15, on June 22, 2006
    *        Control building safety related cable tray area and stairway Number 3, Fire Area
              C-16 and C-29, on June 22, 2006
    *        Division I EDG control and diesel engine rooms, Fire Area DG-6/Z-1, on June 22,
              2006
    Documents reviewed by the inspectors included:
    *        Pre-Fire Plan/Strategy Book
    *        USAR Section 9A.2, Fire Hazards Analysis, Revision 10
    *        River Bend Station postfire safe shutdown analysis
    *        RBNP-038, Site Fire Protection Program, Revision 6B
    The inspectors completed six inspection samples.
  b. Findings
    No findings of significance were identified.
1R08 Inservice Inspection Activities
  a. Inspection Scope
    The inspector witnessed the performance of 12 volumetric (ultrasonic) and four surface
    (liquid penetrant) examinations. The sample of nondestructive examination (NDE)
    activities is listed in the attachment.
    For each of the NDE activities reviewed, the inspector verified that the examinations
    were performed in accordance with American Society of Mechanical Engineers (ASME)
    Code requirements.
                                              -8-                                      Enclosure
 
    During the review of each examination, the inspector verified that appropriate NDE
    procedures were used, that examinations and conditions were as specified in the
    procedure, and that test instrumentation or equipment was properly calibrated and within
    the allowable calibration period. The inspector also reviewed documentation to verify
    that indications revealed by the examinations were dispositioned in accordance with the
    ASME Code specified acceptance standards.
    The inspector verified the certifications of the NDE personnel observed performing
    examinations or identified during review of completed examination packages.
    The inspection procedure requires review of one or two examinations from the previous
    outage with recordable indications that were accepted for continued service to ensure
    that the disposition was done in accordance with the ASME Code. There were no
    recordable indications that required evaluation during the last outage.
    If the licensee completed welding on the pressure boundary for Class 1 or 2 systems
    since the beginning of the previous outage, the procedure requires verification that
    acceptance and preservice examinations were done in accordance with the ASME Code
    for one to three welds. There were no welds available for review.
    The procedure also requires verification that one or two ASME Code Section XI repairs
    or replacements meet code requirements. There were no code repairs or replacements
    available at the time of this inspection.
    The inspectors completed 16 inspection samples.
  b. Findings
    No findings of significance were identified.
1R11 Licensed Operator Requalification Program
  a. Inspection Scope
    On June 13, 2006, the inspectors observed testing and training of senior reactor
    operators and reactor operators to verify the adequacy of training, to assess operator
    performance, and to assess the evaluators critique. The training evaluation scenario
    observed was RSMS-OPS-422, Loss of Circ Water Pump, Failure of Steam Flow
    Transmitter and Instrument Air System Leak, Revision 4.
    The inspectors completed one inspection sample.
  b. Findings
    No findings of significance were identified.
                                              -9-                                  Enclosure
 
1R12 Maintenance Effectiveness
  a. Inspection Scope
    The inspectors reviewed the condition reports (CR) listed below which documented
    equipment problems to: (1) verify the appropriate handling of structure, system, and
    component (SSC) performance or condition problems; (2) verify the appropriate
    handling of degraded SSC functional performance; (3) evaluate the role of work
    practices and common cause problems; and (4) evaluate the handling of SSC issues
    reviewed under the requirements of the maintenance rule; 10 CFR Part 50, Appendix B;
    and TS.
    *      CR-RBS-2006-1898, main steam stop Valve B21-MOVF098C leakage, reviewed
            on June 2, 2006, and CR-RBS-2004-4338, main steam stop Valve B21-
            MOVF098C high leakage during RFO-11 and -12, reviewed on June 26, 2006.
    *      CR-RBS-2006-2302, primary containment integrity maintenance rule repetitive
            functional failure, reviewed on June 26, 2006.
    Documents reviewed by the inspectors included:
    *      NUMARC 93-01, Nuclear Energy Institute Industry (NEI) Guideline for Monitoring
            the Effectiveness of Maintenance at Nuclear Power Plants, Revision 2
    *      Maintenance rule function list
    *      Maintenance rule performance criteria list
    *      Main steam stop valve maintenance rule performance evaluations
    The inspectors completed two inspection samples.
  b. Findings
    No findings of significance were identified.
1R13 Maintenance Risk Assessments and Emergent Work Control
  a. Inspection Scope
  .1 Risk Assessment and Management of Risk
    The inspectors reviewed the planned work weeks listed below to verify: (1) that the
    licensee performed risk assessments when required by 10 CFR 50.65 (a)(4) and
    administrative Procedure ADM-096, Risk Management Program Implementation and
    On-Line Maintenance Risk Assessment, Revision 4B, prior to changes in plant
    configuration for maintenance activities and plant operations; (2) the accuracy,
    adequacy, and completeness of the information considered in the risk assessment;
                                            -10-                                  Enclosure
 
      (3) that the licensee recognized, and entered as applicable, the appropriate licensee
      established risk category according to the risk assessment results and Procedure ADM-
      096; and (4) that the licensee identified and corrected problems related to maintenance
      risk assessments. Specific work activities evaluated included planned and emergent
      work for the weeks of:
      *        June 5, 2006, Division I work week and preferred station service Transformer
              RTX-ESR1F cooling oil dehydration
      *        June 19, 2006, planned Division II EDG outage week
      *        June 26, 2006, nondivisional work week and potential labor work stoppage
  .2 Emergent Work Control
      For the two emergent work activities listed below, the inspectors: (1) verified that the
      licensee performed actions to minimize the probability of initiating events and
      maintained the functional capability of mitigating systems and barrier integrity systems;
      (2) verified that emergent work related activities such as troubleshooting, work
      planning/scheduling, establishing plant conditions, aligning equipment, tagging,
      temporary modifications, and equipment restoration did not place the plant in an
      unacceptable configuration; and (3) reviewed the CAP to determine if the licensee
      identified and corrected risk assessment and emergent work control problems.
      *        Preferred station service Transformer RTX-ESR1F sudden pressure relay failure
              on May 30, 2006
      *        Main turbine bypass valves inoperable due to hydraulic oil leak on June 2, 2006
      The inspectors completed five inspection samples.
  c. Findings
      No findings of significance were identified.
1R14 Operator Performance During Nonroutine Evolutions and Events
  a. Inspection Scope
  1.  April 4, 2006, Automatic Initiation of Standby Service Water
      The inspectors: (1) reviewed operator logs, plant computer data, and strip charts for the
      April 4, 2006, unexpected initiation of Division II standby service water that occurred
      while swapping the running normal service water pumps to evaluate operator
      performance in coping with the event; (2) verified that operator actions were in
      accordance with the response required by plant procedures and training; and (3) verified
      that the licensee identified and implemented appropriate corrective actions associated
      with personnel performance problems that occurred during the transient. In addition, the
                                              -11-                                    Enclosure
 
      inspectors reviewed CR-RBS-2006-01257, which documented the procedural problems
      that led to the event and reviewed the following procedures used by the operators:
      *      AOP-53, Initiation of Standby Service Water With Normal Service Water
              Running, Revision 8
      *      SOP-42, Standby Service Water System, Revision 25
      *      SOP-66, Control Building HVAC Chilled Water System, Revision 33B
  2.  April 15, 2006, Reactor Scram
      The inspectors: (1) reviewed operator logs, plant computer data, and strip charts for the
      April 15, 2006, unexpected reactor recirculation pump downshift and subsequent reactor
      scram to evaluate operator performance in coping with the event; (2) verified that
      operator actions were in accordance with the response required by plant procedures
      and training; and (3) verified that the licensee identified and implemented appropriate
      corrective actions associated with personnel performance problems that occurred during
      the transient. In addition the inspectors reviewed the postscram report documented in
      Procedure GOP-003, Scram Recovery, Revision 16A, and observed the onsite safety
      review committee review of the postscram report.
      The inspectors completed two inspection samples.
  e. Findings
      No findings of significance were identified.
1R15 Operability Evaluations
  a. Inspection Scope
      For the operability evaluations associated with the documents listed below, the
      inspectors: (1) reviewed plants status documents such as operator shift logs, emergent
      work documentation, deferred modifications, and standing orders, to determine if an
      operability evaluation was warranted for degraded components; (2) referred to the
      USAR and design basis documents to review the technical adequacy of licensee
      operability evaluations; (3) evaluated compensatory measures associated with
      operability evaluations; (4) determined degraded component impact on any TS; (5) used
      the significance determination process to evaluate the risk significance of degraded or
      inoperable equipment; and (6) verified that the licensee identified and implemented
      appropriate corrective actions associated with degraded components.
      *      CR-RBS-2006-01207 and -01215, Primary containment purge exhaust line fails
              to meet leak rate acceptance criteria, reviewed during the week of April 3, 2006
                                                -12-                                Enclosure
 
  *      CR-RBS-2005-02805, Inserted control Rod 24-29 control blade lifetime
          calculation revised for extended operating cycle, reviewed during the week of
          April 17, 2006
  *      Work Request (WR) 76625, NNS-ACB23 control power light out, suspect bad
          socket, reviewed during the week of May 29, 2006
  *      TS-LCO-06-0711, Division II EDG Generator Output Breaker charging springs
          did not charge during tagout restoration, reviewed on June 23, 2006
  *      CR-RBS-2006-01257, Division II standby service water start on low service water
          pressure, reviewed on June 28, 2006
  *      CR-RBS-2006-02632, turbine bypass valves hydraulic oil leak, reviewed on
          June 28, 2006
  Other documents reviewed by the inspectors are listed in the attachment.
  The inspectors completed six inspection samples.
b. Findings
  Introduction: The inspectors reviewed a self-revealing noncited violation (NCV) of
  10 CFR Part 50, Appendix B, Criterion XVI, "Corrective Action," involving the failure of
  the licensee to identify that the normal supply breaker to the Division III 4.16 kV
  engineered safety features (ESF) bus was not properly racked in following maintenance.
  Description: Following the completion of planned maintenance on Switchgear NNS-
  SWG1A on April 29, 2006, operators were assigned to clear equipment tags and restore
  the system alignment. As part of this task, operators racked in Breaker NNS-ACB23,
  the normal supply breaker to 4.16 kV Switchgear NNS-SWG1C. No actions, such as
  cycling the breaker, were required to verify that the breaker was properly racked in.
  On May 9, 2006, after noting that the control power light associated with Breaker NNS-
  ACB23 was not lit, operators wrote WR 76625 to repair the light. The WR stated that
  the white control power light on Control Room Panel H13-P808 was out with the breaker
  racked in and the control power fuses installed. The WR also indicated that the
  suspected cause was a bad socket and that position Switch 52H had failed in the past to
  make up during closure. A work control center senior reactor operator determined that
  an operability evaluation was not required for the condition described in WR 76625. The
  WR was classified 4D, which indicated that it should be scheduled as resources
  allowed within the normal 16-week work planning schedule. The inspectors noted the
  licensee did not write a CR. The white control power light provides indication that the
  breaker is functional, specifically, that: (1) there is no electrical fault on the line or load
  side of the breaker, (2) the breaker Lockout button is not depressed on Panel 808, and
  (3) the breaker is fully racked into the switchgear. On May 9, 2006, there were no
  electrical faults on Breaker NNS-ACB23 and the Lockout was reset on Panel 808.
                                            -13-                                       Enclosure
 
On May 22, 2006, while aligning Switchgear NNS-SWG1C and the Division III 4.16 kV
ESF bus to the Transformer RSS1 offsite power supply, Breaker NNS-ACB23 failed to
close. Operators racked the breaker out and in, but the breaker failed to close on the
second attempt. Subsequent troubleshooting identified that the breaker had not been
fully racked in as electricians were able to rotate the racking device one additional turn.
The white light on Panel 808 came on and the breaker was successfully closed. The
operators and electricians determined that Breaker NNS-ACB23 had not been not
operators and electricians determined that Breaker NNS-ACB23 had not been not
properly racked in, wrote CR-RBS-2006-02325 and -02337 and initiated WR 77478 to
properly racked in, wrote CR-RBS-2006-02325 and -02337 and initiated WR 77478 to
investigate the problem with racking in Breaker NNS-ACB23. On May 25, 2006, the inspectors questioned the impact that the failure of the breaker toclose had on the licensee's compliance with TS. Specifically, TS 3.8.1.a requires two
investigate the problem with racking in Breaker NNS-ACB23.
On May 25, 2006, the inspectors questioned the impact that the failure of the breaker to
close had on the licensees compliance with TS. Specifically, TS 3.8.1.a requires two
qualified circuits between the offsite transmission network and the onsite Class 1E ac
qualified circuits between the offsite transmission network and the onsite Class 1E ac
electrical power distribution system when the plant is in Modes 1, 2, and 3. On May 12,the plant was taken from Mode 4 to Mode 2 without two qualified offsite power sources
electrical power distribution system when the plant is in Modes 1, 2, and 3. On May 12,
available to the Division III 4.16 kV ESF bus. The licensee wrote CR-RBS-2006-2402and determined that they did not comply with TS 3.8.1.a when they changed modes onMay 12. In addition, the Division III 4.16 kV ESF bus was inoperable for a period of10 days (May 12-22), which exceeded the allowed outage time of 72 hours specified in
the plant was taken from Mode 4 to Mode 2 without two qualified offsite power sources
TS Condition 3.8.1.A. The licensee also discovered that, on May 14 during the conduct
available to the Division III 4.16 kV ESF bus. The licensee wrote CR-RBS-2006-2402
and determined that they did not comply with TS 3.8.1.a when they changed modes on
May 12. In addition, the Division III 4.16 kV ESF bus was inoperable for a period of
10 days (May 12-22), which exceeded the allowed outage time of 72 hours specified in
TS Condition 3.8.1.A. The licensee also discovered that, on May 14 during the conduct
of maintenance on the Division I EDG, with Breaker NNS-ACB23 unable to be closed,
of maintenance on the Division I EDG, with Breaker NNS-ACB23 unable to be closed,
they unknowingly entered TS Condition 3.8.1.d. TS Condition 3.8.1.d states that with"One required offsite circuit inoperable AND on required [E]DG inoperable," restore the
they unknowingly entered TS Condition 3.8.1.d. TS Condition 3.8.1.d states that with
One required offsite circuit inoperable AND on required [E]DG inoperable, restore the
EDG or the offsite power supply to an operable status in 12 hours or place the plant in
EDG or the offsite power supply to an operable status in 12 hours or place the plant in
Mode 3 within the next 12 hours. The Division I EDG was inoperable for 15 hours and
Mode 3 within the next 12 hours. The Division I EDG was inoperable for 15 hours and
15 minutes.The inspectors found that the licensee's procedures did not require Breaker NNS-ACB23 to be cycled to verify proper operation after it was racked in on April 29. Procedure OSP-0022, "Operations General Administrative Guidelines," Revision 01,
15 minutes.
step 4.5.5, required that breakers be functionally tested "following any activity involving
The inspectors found that the licensees procedures did not require Breaker NNS-
safety related equipment which requires the breaker to be racked out.Because
ACB23 to be cycled to verify proper operation after it was racked in on April 29.
Procedure OSP-0022, Operations General Administrative Guidelines, Revision 01,
step 4.5.5, required that breakers be functionally tested following any activity involving
safety related equipment which requires the breaker to be racked out. Because
Breaker NNS-ACB23 is not classified as a safety-related breaker, it was not required to
Breaker NNS-ACB23 is not classified as a safety-related breaker, it was not required to
be functionally tested after it was racked in on April 29. Analysis: The performance deficiency associated with this finding involved the failure ofoperators to identify that Breaker NNS-ACB23 was not functional on April 29, 2006. Thefinding was more than minor because it was associated with the mitigating systemcornerstone attribute of configuration control and affected the associated cornerstone
be functionally tested after it was racked in on April 29.
objective to ensure the availability, reliability, and capability of systems that res
Analysis: The performance deficiency associated with this finding involved the failure of
pond toinitiating events to prevent undesirable consequences. The Phase 1 worksheets in
operators to identify that Breaker NNS-ACB23 was not functional on April 29, 2006. The
finding was more than minor because it was associated with the mitigating system
cornerstone attribute of configuration control and affected the associated cornerstone
objective to ensure the availability, reliability, and capability of systems that respond to
initiating events to prevent undesirable consequences. The Phase 1 worksheets in
Manual Chapter (MC) 0609, "Significance Determination Process," were used to
Manual Chapter (MC) 0609, "Significance Determination Process," were used to
conclude that a Phase 2 analysis was required because both the mitigating systems andthe containment barrier cornerstones were affected. In accordance with NRC Inspection Manual Chapter 0609, Appendix A, Attachment 1,"User Guidance for Determining the Significance of Reactor Inspection Findings for
conclude that a Phase 2 analysis was required because both the mitigating systems and
At-Power Situations," the inspectors estimated the risk of the subject finding using the  
the containment barrier cornerstones were affected.
Enclosure-15-Risk-Informed Inspection Notebook for River Bend Station, Revision 2. The inspectorsassumed that Division III power was available, but degraded, while Breaker NNS-ACB23was not properly installed for the 10 days that the plant was in Mode 3 or above, fromMay 12-22, 2006. Therefore, the exposure window used was 3-30 days. No operator
In accordance with NRC Inspection Manual Chapter 0609, Appendix A, Attachment 1,
"User Guidance for Determining the Significance of Reactor Inspection Findings for
At-Power Situations," the inspectors estimated the risk of the subject finding using the
                                          -14-                                     Enclosure
 
Risk-Informed Inspection Notebook for River Bend Station, Revision 2. The inspectors
assumed that Division III power was available, but degraded, while Breaker NNS-ACB23
was not properly installed for the 10 days that the plant was in Mode 3 or above, from
May 12-22, 2006. Therefore, the exposure window used was 3-30 days. No operator
recovery was credited because on two occasions, operators had proven incapable of
recovery was credited because on two occasions, operators had proven incapable of
properly positioning the breaker, ultimately requiring maintenance technicians to
properly positioning the breaker, ultimately requiring maintenance technicians to
properly install the breaker. Using Manual Chapter 0609, Appendix A, Attachment 2,
properly install the breaker. Using Manual Chapter 0609, Appendix A, Attachment 2,
Rule 2.1, "Inspection Finding that Degrades Mitigation Capability and Does Not ReduceRemaining Mitigation Capability Credit to a Value Less Than Full Mitigation Credit," theinspectors determined that all sequences containing the functions that would be affectedby a loss of Division III power, including the Division I standby service water loop(HPCS, LPI, CHR, HPCS/LC, and REC/SSW), should be quantified, giving full mitigationcapability credit to each of these functions. Because the performance deficiencyaffected the electric power system, Table 2 of the risk-informed notebook required thatall worksheets be evaluated. The resulting dominant sequences are provided in Table 1
Rule 2.1, Inspection Finding that Degrades Mitigation Capability and Does Not Reduce
below:Table 1Phase 2 Worksheet ResultsInitiatorSequenceIELMitigating FunctionsResultTNSW53SSW - REC/SSW7*43RCIC - HPCS - DEP9*LOOP13CHR - LDEP823CHR - SPCFAN8
Remaining Mitigation Capability Credit to a Value Less Than Full Mitigation Credit, the
43RCIC - HPCS - DEP9*63EAC1&2 - HPCS - REC6 - FPW 9*83EAC1&2 - HPCS - SBODG - REC4 9*
inspectors determined that all sequences containing the functions that would be affected
93EAC1&2 - REC1 - HPCS -RCIC9*SORV13CHR-LDEP823CHR - SPCFAN943RCIC - HPCS - DEP9*LOIA24CHR - SPCFAN814CHR-LDEP9TPCS42RCIC - HPCS - DEP8ATWS16CHR9    * Denotes sequences indicated as LERF contributors in the Phase 2 notebook.By application of the counting rule, the internal event risk contribution of this finding tothe change in core damage frequency (CDF) was determined to be of low to moderaterisk significance (WHITE).A senior reactor analyst performed further evaluation of the risk associated with thisissue (Phase 3/Modified Phase 2). Because the assumptions made during the Phase 2
by a loss of Division III power, including the Division I standby service water loop
(HPCS, LPI, CHR, HPCS/LC, and REC/SSW), should be quantified, giving full mitigation
capability credit to each of these functions. Because the performance deficiency
affected the electric power system, Table 2 of the risk-informed notebook required that
all worksheets be evaluated. The resulting dominant sequences are provided in Table 1
below:
                                                              Table 1
                                                  Phase 2 Worksheet Results
    Initiator      Sequence            IEL                      Mitigating Functions  Result
    TNSW              5                3                        SSW - REC/SSW        7*
                        4                3                        RCIC - HPCS - DEP      9*
                        1                3                            CHR - LDEP          8
                        2                3                          CHR - SPCFAN          8
    LOOP              4                3                        RCIC - HPCS - DEP      9*
                        6                3                  EAC1&2 - HPCS - REC6 - FPW   9*
                        8                3                EAC1&2 - HPCS - SBODG - REC4 9*
                        9                3                  EAC1&2 - REC1 - HPCS -RCIC  9*
                        1                3                            CHR-LDEP          8
    SORV              2                3                          CHR - SPCFAN          9
                        4                3                        RCIC - HPCS - DEP      9*
                        2                4                          CHR - SPCFAN          8
      LOIA
                        1                4                            CHR-LDEP          9
    TPCS              4                2                        RCIC - HPCS - DEP      8
    ATWS              1                6                                CHR            9
    * Denotes sequences indicated as LERF contributors in the Phase 2 notebook.
By application of the counting rule, the internal event risk contribution of this finding to
the change in core damage frequency (CDF) was determined to be of low to moderate
risk significance (WHITE).
A senior reactor analyst performed further evaluation of the risk associated with this
issue (Phase 3/Modified Phase 2). Because the assumptions made during the Phase 2
estimation process were overly conservative and did not completely represent the actual
estimation process were overly conservative and did not completely represent the actual
exposure time nor the actual affect the performance deficiency had on the availability ofpower to the Division III diesel generator, the senior reactor analyst modified these  
exposure time nor the actual affect the performance deficiency had on the availability of
Enclosure-16-assumptions to more precisely quantify the change in risk. Specifically, the exposuretime was 10 days as opposed to the 30 days used in the risk-informed notebook.  
power to the Division III diesel generator, the senior reactor analyst modified these
                                                        -15-                               Enclosure
 
assumptions to more precisely quantify the change in risk. Specifically, the exposure
time was 10 days as opposed to the 30 days used in the risk-informed notebook.
Additionally, the Phase 2 evaluation included loss of offsite power initiating events that
Additionally, the Phase 2 evaluation included loss of offsite power initiating events that
were not affected by the performance deficiency because offsite power to Division III
were not affected by the performance deficiency because offsite power to Division III
would in all likelihood be lost during a design basis loss of offsite power. The senior
would in all likelihood be lost during a design basis loss of offsite power. The senior
reactor analyst performed a modified Phase 2 estimation and determined that the
reactor analyst performed a modified Phase 2 estimation and determined that the
internal event risk contribution of the subject finding to the CDF was of very low risksignificance (Green). The best estimate value of this probability (CDFINTERNAL) wascalculated by the senior reactor analyst to be 1.2 x 10
internal event risk contribution of the subject finding to the CDF was of very low risk
-7. The analyst evaluated thecontribution of external initiating events to the risk and calculated a bounding risk
significance (Green). The best estimate value of this probability (CDFINTERNAL) was
estimate of 2.9 x 10
calculated by the senior reactor analyst to be 1.2 x 10-7. The analyst evaluated the
-7 as the CDF for internal fire events.Using Manual Chapter 0609, Appendix H, "Containment Integrity SignificanceDetermination Process," the analyst estimated that the potential risk contribution fromlarge early release frequency was 6.6 x 10
contribution of external initiating events to the risk and calculated a bounding risk
-8.Given the independence of each initiating event, the analyst determined that the bestestimate of the total risk related to the subject performance deficiency was the
estimate of 2.9 x 10-7 as the CDF for internal fire events.
summation of the CDF calculated for both internal and external initiators. Therefore,the best estimate was 4.1 x 10
Using Manual Chapter 0609, Appendix H, Containment Integrity Significance
-7. The change in risk related to large early releasefrequency was determined to be below 6.6 x 10
Determination Process, the analyst estimated that the potential risk contribution from
-8, corroborating that the finding was ofvery low risk significance. The performance deficiency resulted in a finding that was of
large early release frequency was 6.6 x 10-8.
very low risk significance (Green). The cause of the finding was related to the
Given the independence of each initiating event, the analyst determined that the best
crosscutting aspect of problem identification and resolution in that operators failed toidentify that Breaker NNS-ACB23 was not properly racked in. Enforcement: 10 CFR Part 50, Appendix B, Criterion XVI, Corrective Action, requires, inpart, that measures be established to assure that conditions adverse to quality are
estimate of the total risk related to the subject performance deficiency was the
promptly identified and corrected. Contrary to this, from April 29 to May 22, 2006, the
summation of the CDF calculated for both internal and external initiators. Therefore,
the best estimate was 4.1 x 10-7. The change in risk related to large early release
frequency was determined to be below 6.6 x 10-8, corroborating that the finding was of
very low risk significance. The performance deficiency resulted in a finding that was of
very low risk significance (Green). The cause of the finding was related to the
crosscutting aspect of problem identification and resolution in that operators failed to
identify that Breaker NNS-ACB23 was not properly racked in.
Enforcement: 10 CFR Part 50, Appendix B, Criterion XVI, Corrective Action, requires, in
part, that measures be established to assure that conditions adverse to quality are
promptly identified and corrected. Contrary to this, from April 29 to May 22, 2006, the
licensee failed to identify that Breaker NNS-ACB23, which supplied one of the two
licensee failed to identify that Breaker NNS-ACB23, which supplied one of the two
required offsite power supplies to the Division III 4.16 kV ESF bus, was not properlyracked in to Switchgear NNS-SWGIC. The root cause involved the licensee's lack of
required offsite power supplies to the Division III 4.16 kV ESF bus, was not properly
racked in to Switchgear NNS-SWGIC. The root cause involved the licensees lack of
understanding that Breaker NNS-ACB23 was required to be functional to meet
understanding that Breaker NNS-ACB23 was required to be functional to meet
TS 3.8.1.a requirements for two offsite power circuits to the Division III 4.16 kV ESFbus. The corrective actions to restore compliance included: (1) changes to operations
TS 3.8.1.a requirements for two offsite power circuits to the Division III 4.16 kV ESF
bus. The corrective actions to restore compliance included: (1) changes to operations
section procedures to verify the white control power light, when applicable, after a circuit
section procedures to verify the white control power light, when applicable, after a circuit
breaker is racked in, (2) expansion of the requirement to functionally test safety-related
breaker is racked in, (2) expansion of the requirement to functionally test safety-related
breakers to the nonsafety-related breakers in the TS required offsite power circuits, and
breakers to the nonsafety-related breakers in the TS required offsite power circuits, and
(3) operator lessons learned training on the event and all of its ramifications. Because
(3) operator lessons learned training on the event and all of its ramifications. Because
the finding was of very low safety significance and has been entered into the licensee's
the finding was of very low safety significance and has been entered into the licensees
CAP as CR-RBS-2006-02402, this violation is being treated as an NCV consistent with
CAP as CR-RBS-2006-02402, this violation is being treated as an NCV consistent with
Section VI.A of the Enforcement Policy: NCV 05000458/2006003-01, "Failure to identify
Section VI.A of the Enforcement Policy: NCV 05000458/2006003-01, Failure to identify
Division III ESF bus supply breaker not racked in."
Division III ESF bus supply breaker not racked in.
Enclosure-17-1R19Postmaintenance Testing     a.Inspection ScopeFor the five postmaintenance test activities of risk significant systems or componentslisted below, the inspectors: (1) reviewed the applicable licensing basis and/or design-
                                          -16-                                   Enclosure
basis documents to determine the safety functions; (2) evaluated the safety functions
 
that may have been affected by the maintenance activity; and (3) reviewed the test
1R19 Postmaintenance Testing
procedure to verify that it adequately tested the safety function that may have been
  a. Inspection Scope
affected. The inspectors either witnessed or reviewed test data to verify that
    For the five postmaintenance test activities of risk significant systems or components
acceptance criteria were met, plant impacts were evaluated, test equipment was
    listed below, the inspectors: (1) reviewed the applicable licensing basis and/or design-
calibrated, procedures were followed, jumpers were properly controlled, the test dataresults were complete and accurate, the test equipment was remo
    basis documents to determine the safety functions; (2) evaluated the safety functions
ved, the system wasproperly re-aligned, and deficiencies during testing were documented. The inspectors
    that may have been affected by the maintenance activity; and (3) reviewed the test
also reviewed the CAP to determine if the licensee identified and corrected problems
    procedure to verify that it adequately tested the safety function that may have been
related to postmaintenance testing. *Work Order (WO) 50370422, Division II battery cell post seal replacement,reviewed during the week of May 8, 2006*WO 87721, replace control Rods 40-37, 44-41, and 48-25 and 12-25 individualscram test switches, reviewed May 19, 2006*WO 69816, low pressure core spray keep fill pump discharge check valve, E21-VF033 replacement, reviewed during the week of June 19, 2006*WO 85194, signature testing on high pressure core spray room unit coolerservice water outlet valve, SWP-MOV74B, reviewed during the week of June 19,
    affected. The inspectors either witnessed or reviewed test data to verify that
2006*WO 90342, Division II EDG generator output Breaker ENS-SWG1B-ACB027charging springs failed to charge during tagout restoration, reviewed on June 23,
    acceptance criteria were met, plant impacts were evaluated, test equipment was
2006The inspectors completed five inspection samples.     g.FindingsNo findings of significance were identified.1R20Refueling and Other Outage Activities     a.Inspection ScopeThe inspectors reviewed the following risk important refueling outage activities to verifydefense in depth commensurate with the outage risk control plan and compliance with
    calibrated, procedures were followed, jumpers were properly controlled, the test data
the TS during RFO-13 from April 23 to May 12, 2006: (1) the risk control plan;
    results were complete and accurate, the test equipment was removed, the system was
(2) tagging/clearance activities; (3) reactor coolant system instrumentation; (4) electrical  
    properly re-aligned, and deficiencies during testing were documented. The inspectors
Enclosure-18-power; (5) decay heat removal; (6) spent fuel pool cooling; (7) inventory control;(8) reactivity control; (9) containment closure; (10) reduced inventory conditions;
    also reviewed the CAP to determine if the licensee identified and corrected problems
(11) refueling activities; (12) heatup and cooldown activities; (13) restart activities; and
    related to postmaintenance testing.
(14) licensee identification and implementation of appropriate corrective actions
    *       Work Order (WO) 50370422, Division II battery cell post seal replacement,
associated with RFO activities. The inspectors' containment inspections included
            reviewed during the week of May 8, 2006
observations of the containment sump for damage and debris, and supports, braces,
    *       WO 87721, replace control Rods 40-37, 44-41, and 48-25 and 12-25 individual
and snubbers for evidence of excessive stress, water hammer, or aging. Specific
            scram test switches, reviewed May 19, 2006
outage activities observed and reviewed included:*Outage risk assessment team (ORAT) report to onsite safety review committee*Reactor shutdown, cooldown, and vessel disassembly
    *       WO 69816, low pressure core spray keep fill pump discharge check valve, E21-
*Refueling operations, fuel sipping, and off loaded fuel inspections
            VF033 replacement, reviewed during the week of June 19, 2006
*Daily/shiftly shutdown operations protection plan assessments
    *       WO 85194, signature testing on high pressure core spray room unit cooler
*Shutdown postscram report to onsite safety review committee
            service water outlet valve, SWP-MOV74B, reviewed during the week of June 19,
*Reactor recirculation pump trip logic modification installation and testing
            2006
*Main steam line local leak rate testing
    *       WO 90342, Division II EDG generator output Breaker ENS-SWG1B-ACB027
*Transformer RSS1 offsite power line equipment inspection and upgrade
            charging springs failed to charge during tagout restoration, reviewed on June 23,
*Division II to Division I protected division swap
            2006
*Infrequently performed test or evolution briefings for:- Divisional loss of offsite power/loss of coolant accident testing
    The inspectors completed five inspection samples.
- Concurrent control rod mechanism and blade changeout
  g. Findings
- Reactor vessel pressure test and scram time testing
    No findings of significance were identified.
- Reactor startup, heatup, and power ascension
1R20 Refueling and Other Outage Activities
- Onsite safety review committee meeting to recommend startup
  a. Inspection Scope
- Drywell 900 psi walkdown (after shutdown and during startup)Documents reviewed by the inspectors are listed in the attachment.
    The inspectors reviewed the following risk important refueling outage activities to verify
The inspectors completed one inspection sample.     b.FindingsIntroduction: An NRC identified NCV of 10 CFR 50.65, "Maintenance Rule,"Section (a)(4) was identified for the failure of the licensee to provide prescribed
    defense in depth commensurate with the outage risk control plan and compliance with
compensatory measures for the highest shutdown risk condition during RFO-13.  
    the TS during RFO-13 from April 23 to May 12, 2006: (1) the risk control plan;
Specifically, the preoutage risk assessment recommended that two WOs be in place for
    (2) tagging/clearance activities; (3) reactor coolant system instrumentation; (4) electrical
maintenance electricians to provide power to one spent fuel pool cooling pump in the
                                              -17-                                   Enclosure
event of problems with the running pump during periods of safety-related electrical bus
 
maintenance. The inspectors found that the WOs were not in place before enteringshutdown risk condition Orange on April 26, 2006, during the Division II ESF bus testing,
  power; (5) decay heat removal; (6) spent fuel pool cooling; (7) inventory control;
and on May 3, 2006, during the Division I ESF bus outage.Description: The inspectors observed the onsite safety review committee meeting todiscuss and approve the ORAT report for RFO-13. The report noted two Orange
  (8) reactivity control; (9) containment closure; (10) reduced inventory conditions;
shutdown risk conditions for spent fuel pool cooling (SFC). Only one SFC pump would
  (11) refueling activities; (12) heatup and cooldown activities; (13) restart activities; and
be available after the beginning of core offload: (1) during the Division II ESF bus
  (14) licensee identification and implementation of appropriate corrective actions
testing with the SFC-P1B breaker racked out, and (2) during the Division I ESF bus
  associated with RFO activities. The inspectors' containment inspections included
outage when SFC-P1A was without power. As a result of the ORAT review of  
  observations of the containment sump for damage and debris, and supports, braces,
Enclosure-19-Procedure AOP-0051, "Loss of Decay Heat Removal," Revision 17, they recommendedthat the planned maintenance optimization group develop WOs for maintenanceelectricians to provide alternate power from the station blackout diesel generator to the
  and snubbers for evidence of excessive stress, water hammer, or aging. Specific
deenergized SFC pump in the event of a failure of the running pump.In addition, Procedure OSP-0037, "Shutdown Operations Protection Plan," Revision 16,Section 4.7, "Fuel Pool Cooling," required that: (1) if work was required on SFC during
  outage activities observed and reviewed included:
the outage, then it should be done as early as possible in the outage and not after fueloffload (when heat load is the highest); and (2) if work was required after fuel offload,
  *       Outage risk assessment team (ORAT) report to onsite safety review committee
then a contingency plan shall be in place prior to removing t
  *       Reactor shutdown, cooldown, and vessel disassembly
he system from service. The inspectors determined that this requirement applied to deenergizing an SFC pump
  *       Refueling operations, fuel sipping, and off loaded fuel inspections
for electrical bus maintenance.On May 3, 2006, during the Division I ESF bus outage, the inspectors asked theoperations shift manager if the required WO was available to provide alternate power to
  *       Daily/shiftly shutdown operations protection plan assessments
SFC-P1A in the event that the running SFC-P1B failed. He stated that he assumed thatthe WO was written and that he would check. The inspectors then requested a copy of
  *       Shutdown postscram report to onsite safety review committee
  *       Reactor recirculation pump trip logic modification installation and testing
  *       Main steam line local leak rate testing
  *       Transformer RSS1 offsite power line equipment inspection and upgrade
  *       Division II to Division I protected division swap
  *       Infrequently performed test or evolution briefings for:
          - Divisional loss of offsite power/loss of coolant accident testing
          - Concurrent control rod mechanism and blade changeout
          - Reactor vessel pressure test and scram time testing
          - Reactor startup, heatup, and power ascension
          - Onsite safety review committee meeting to recommend startup
          - Drywell 900 psi walkdown (after shutdown and during startup)
  Documents reviewed by the inspectors are listed in the attachment.
  The inspectors completed one inspection sample.
b. Findings
  Introduction: An NRC identified NCV of 10 CFR 50.65, Maintenance Rule,
  Section (a)(4) was identified for the failure of the licensee to provide prescribed
  compensatory measures for the highest shutdown risk condition during RFO-13.
  Specifically, the preoutage risk assessment recommended that two WOs be in place for
  maintenance electricians to provide power to one spent fuel pool cooling pump in the
  event of problems with the running pump during periods of safety-related electrical bus
  maintenance. The inspectors found that the WOs were not in place before entering
  shutdown risk condition Orange on April 26, 2006, during the Division II ESF bus testing,
  and on May 3, 2006, during the Division I ESF bus outage.
  Description: The inspectors observed the onsite safety review committee meeting to
  discuss and approve the ORAT report for RFO-13. The report noted two Orange
  shutdown risk conditions for spent fuel pool cooling (SFC). Only one SFC pump would
  be available after the beginning of core offload: (1) during the Division II ESF bus
  testing with the SFC-P1B breaker racked out, and (2) during the Division I ESF bus
  outage when SFC-P1A was without power. As a result of the ORAT review of
                                            -18-                                     Enclosure
 
Procedure AOP-0051, Loss of Decay Heat Removal, Revision 17, they recommended
that the planned maintenance optimization group develop WOs for maintenance
electricians to provide alternate power from the station blackout diesel generator to the
deenergized SFC pump in the event of a failure of the running pump.
In addition, Procedure OSP-0037, Shutdown Operations Protection Plan, Revision 16,
Section 4.7, Fuel Pool Cooling, required that: (1) if work was required on SFC during
the outage, then it should be done as early as possible in the outage and not after fuel
offload (when heat load is the highest); and (2) if work was required after fuel offload,
then a contingency plan shall be in place prior to removing the system from service.
The inspectors determined that this requirement applied to deenergizing an SFC pump
for electrical bus maintenance.
On May 3, 2006, during the Division I ESF bus outage, the inspectors asked the
operations shift manager if the required WO was available to provide alternate power to
SFC-P1A in the event that the running SFC-P1B failed. He stated that he assumed that
the WO was written and that he would check. The inspectors then requested a copy of
the WO and a senior work planner reported that the WO was not available since it was
the WO and a senior work planner reported that the WO was not available since it was
not yet approved for use in the electronic work planning program. Following discussions
not yet approved for use in the electronic work planning program. Following discussions
with operators in the work management center, the licensee immediately took actions toensure that both WOs were processed and made ready for use.The inspectors reviewed AOP-0051, Attachment 1, "Spent Fuel Pool Curves," anddetermined that the approximate "time to boil" for the spent fuel pool at that time withoffload fuel in the pool was approximately 8 hours. Based on that data and the time
with operators in the work management center, the licensee immediately took actions to
needed to generate the WOs, the inspectors determined that there was adequate timefor the licensee to connect an alternate power supply to the SFC pumps before the
ensure that both WOs were processed and made ready for use.
spent fuel pool water started to boil if there was a failure of the running pump.Analysis: The performance deficiency associated with this finding involved the failure toestablish prescribed compensatory measures for the highest outage risk condition
The inspectors reviewed AOP-0051, Attachment 1, Spent Fuel Pool Curves, and
during RFO-13 as required by the shutdown operations protection plan. The finding was
determined that the approximate time to boil for the spent fuel pool at that time with
offload fuel in the pool was approximately 8 hours. Based on that data and the time
needed to generate the WOs, the inspectors determined that there was adequate time
for the licensee to connect an alternate power supply to the SFC pumps before the
spent fuel pool water started to boil if there was a failure of the running pump.
Analysis: The performance deficiency associated with this finding involved the failure to
establish prescribed compensatory measures for the highest outage risk condition
during RFO-13 as required by the shutdown operations protection plan. The finding was
more than minor because the licensee failed to implement prescribed compensatory
more than minor because the licensee failed to implement prescribed compensatory
measures and failed to effectively manage those measures. The finding affected the
measures and failed to effectively manage those measures. The finding affected the
mitigating system cornerstone because of the increased risk of a sustained loss of SFCduring core offloading operations. The finding could not be evaluated using the
mitigating system cornerstone because of the increased risk of a sustained loss of SFC
during core offloading operations. The finding could not be evaluated using the
significance determination process; therefore, the finding was reviewed by regional
significance determination process; therefore, the finding was reviewed by regional
management and determined to be of very low safety significance. Factors that were
management and determined to be of very low safety significance. Factors that were
considered included: (1) electrical maintenance technicians had previously performed
considered included: (1) electrical maintenance technicians had previously performed
the task of providing alternate power to an SFC pump, (2) the necessary equipment was
the task of providing alternate power to an SFC pump, (2) the necessary equipment was
staged as part of the abnormal operating procedure for loss of decay heat removal, and
staged as part of the abnormal operating procedure for loss of decay heat removal, and
(3) the relatively long "time to boil" of the spent fuel storage pool at that time during the
(3) the relatively long time to boil of the spent fuel storage pool at that time during the
refueling outage. The cause of the finding was related to the cro
refueling outage. The cause of the finding was related to the crosscutting aspect of
sscutti ng aspect ofhuman performance because the licensee's planned maintenance activities and the
human performance because the licensees planned maintenance activities and the
predetermined increase in outage risk was not effectively managed by prescribed
predetermined increase in outage risk was not effectively managed by prescribed
compensatory measures.  
compensatory measures.
Enclosure-20-Enforcement: 10 CFR 50.65(a)(4) requires, in part, that before performing maintenanceactivities, the licensee shall assess and manage the increase in risk that may result from
                                          -19-                                     Enclosure
the proposed maintenance activities. Contrary to this, the licensee failed to properly
 
manage the highest outage risk condition of RFO-13. On April 26, 2006, the plant
    Enforcement: 10 CFR 50.65(a)(4) requires, in part, that before performing maintenance
entered an Orange outage risk condition for SFC during core offload, when SFC-P1B
    activities, the licensee shall assess and manage the increase in risk that may result from
was deenergized for Division II ESF bus testing. On May 3, 2006, the plant entered an
    the proposed maintenance activities. Contrary to this, the licensee failed to properly
Orange outage risk condition for SFC during core offload, when SFC-P1A was
    manage the highest outage risk condition of RFO-13. On April 26, 2006, the plant
deenergized for a Division I ESF bus outage. WOs were not written and ready for use
    entered an Orange outage risk condition for SFC during core offload, when SFC-P1B
to have electricians provide alternate power to an SFC pump in the event the running
    was deenergized for Division II ESF bus testing. On May 3, 2006, the plant entered an
pump failed. The root cause involved the failure of the licensee to ensure that the WOwas in place before the plant entered the Orange shutdown risk condition. Corrective
    Orange outage risk condition for SFC during core offload, when SFC-P1A was
action was taken to process the WOs for immediate use. Because the finding was of
    deenergized for a Division I ESF bus outage. WOs were not written and ready for use
very low safety significance and was entered into the licensee's CAP as CR-RBS-2006-
    to have electricians provide alternate power to an SFC pump in the event the running
01937, this violation is being treated as an NCV consistent with Section VI.A of the
    pump failed. The root cause involved the failure of the licensee to ensure that the WO
Enforcement Policy: NCV 05000458/2006003-02, "Failure to adequately manage an
    was in place before the plant entered the Orange shutdown risk condition. Corrective
increase in plant risk." 1R22Surveillance Testing     a.Inspection ScopeThe inspectors reviewed the USAR, procedure requirements, and TS to ensure that thesix surveillance activities listed below demonstrated that the SSCs tested were capable
    action was taken to process the WOs for immediate use. Because the finding was of
of performing their intended safety functions. The inspectors either witnessed or
    very low safety significance and was entered into the licensees CAP as CR-RBS-2006-
reviewed test data to verify that the following significant surveillance test attributes were
    01937, this violation is being treated as an NCV consistent with Section VI.A of the
adequate: (1) preconditioning; (2) evaluation of testing impact on the plant;
    Enforcement Policy: NCV 05000458/2006003-02, "Failure to adequately manage an
(3) acceptance criteria; (4) test equipment; (5) procedures; (6) jumper/lifted lead
    increase in plant risk."
controls; (7) test data; (8) testing frequency and method demonstrated TS operability;(9) test equipment removal; (10) restoration of plant systems; (11) fulfillment of ASMECode requirements; (12) updating of performance indicator (PI) data; (13) engineering
1R22 Surveillance Testing
evaluations, root causes, and bases for returning tested SSCs not meeting the test
  a. Inspection Scope
acceptance criteria were correct; (14) reference setting data; and (15) annunciator and
    The inspectors reviewed the USAR, procedure requirements, and TS to ensure that the
alarm setpoints. The inspectors also verified that the licensee identified and
    six surveillance activities listed below demonstrated that the SSCs tested were capable
implemented any needed corrective actions associated with the surveillance testing. *STP-208-3601, "'A' Main Steam Line MSIV's and Outboard Drain Valve LeakRate Test and Inboard MSIV Inleakage Test," Revision 6, performed on May 2,
    of performing their intended safety functions. The inspectors either witnessed or
2006*STP-305-1606, "[Division I Battery] ENB-BAT1A Service Discharge Test,"Revision 17, performed on May 6, 2006*STP-050-3601, "Shutdown Margin Demonstration," Revision 27, performed onMay 12, 2006*STP-000-0102, "Power Distribution Alignment Check," Revision 5, performed onMay 14 and 15, 2006  
    reviewed test data to verify that the following significant surveillance test attributes were
Enclosure-21-*STP-508-4543, "Turbine First Stage Pressure Channel Functional Test,"Revision 7, performed on June 4, 2006*Reactor coolant sample using Procedures COP-0001, "Sampling via VariousBalance-Of-Plant Systems," Attachment 8, "Reactor Sample Panel Routine
    adequate: (1) preconditioning; (2) evaluation of testing impact on the plant;
Sample Points," Revision 14, and COP-0305, "Operation of the Countroom
    (3) acceptance criteria; (4) test equipment; (5) procedures; (6) jumper/lifted lead
Analysis Systems," Revision 2, performed on June 15, 2006Documents reviewed by the inspectors are listed in the attachment.
    controls; (7) test data; (8) testing frequency and method demonstrated TS operability;
The inspectors completed six inspection samples.     h.FindingsIntroduction: The inspectors identified an NCV of TS 5.4.1.a for the failure of thelicensee to provide an adequate surveillance test procedure to perform TS SurveillanceRequirement (SR) 3.8.1.1. Specifically, STP-000-0102, "Power Distribution AlignmentCheck," Revision 4, did not include steps to verify the required offsite power circuit
    (9) test equipment removal; (10) restoration of plant systems; (11) fulfillment of ASME
breaker alignment and indicated power availability for the Division III 4.16 kV ESF bus as required in Modes 1, 2, and 3. Description: As discussed in Section 1R15 of this report, operators failed to properlyrack in Breaker NNS-ACB23 on April 29, 2006. This condition was discovered on
    Code requirements; (12) updating of performance indicator (PI) data; (13) engineering
May 22, when the breaker failed to close. During this period, on May 14, 2006, the
    evaluations, root causes, and bases for returning tested SSCs not meeting the test
Division I EDG was removed from service to replace a leaking section of jacket cooling
    acceptance criteria were correct; (14) reference setting data; and (15) annunciator and
water vent tubing. With the Division I EDG removed from service, TS Required
    alarm setpoints. The inspectors also verified that the licensee identified and
Action 3.8.1.a.1 required that operators perform TS SR 3.8.1.1 within one hour andonce every 8 hours until the EDG was operable. TS SR 3.8.1.1 required operators toverify the correct breaker alignment and indicated power for each required offsite power
    implemented any needed corrective actions associated with the surveillance testing.
circuit. Operators utilized Procedure STP-000-0102, "Power Distribution AlignmentCheck," Revision 4, to satisfy the requirements of TS SR 3.8.1.1; however, the
    *       STP-208-3601, "A Main Steam Line MSIVs and Outboard Drain Valve Leak
inspectors identified that the procedure did not have steps to verify the correct breaker
              Rate Test and Inboard MSIV Inleakage Test," Revision 6, performed on May 2,
alignment and indicated power availability to the Division III 4.16 kV ESF bus. As aresult, the operators did not identify that Breaker NNS-ACB23 was not racked in. During the period that the Division I EDG was removed from service, the plant wasactually in TS Condition 3.8.1.d. TS Condition 3.8.1.d states that with "One requiredoffsite circuit inoperable AND one required [E]DG inoperable," restore the EDG or the
              2006
offsite power supply to an operable status in 12 hours or place the plant in Mode 3 within
    *       STP-305-1606, [Division I Battery] ENB-BAT1A Service Discharge Test,
the next 12 hours. The Division I EDG was inoperable for 15 hours and 15 minutes.Procedure STP-000-0102, Section 1.1, states, in part, that its purpose is to verify thecorrect breaker alignment and indicated power availability for each required offsitepower circuit in accordance with TS SR 3.8.1.1 in Modes 1, 2, and 3. TS 3.8.1 basesdefines an offsite power circuit as follows: "Each offsite circuit consists of incoming
              Revision 17, performed on May 6, 2006
breakers and disconnects to the respective preferred station service Transformers 1C
    *       STP-050-3601, Shutdown Margin Demonstration, Revision 27, performed on
and 1D [RSS1 and RSS2], the 1C and 1D preferred station service transformers, and
              May 12, 2006
the respective circuit path including feeder breakers to the three 4.16 kV ESF buses.
    *       STP-000-0102, Power Distribution Alignment Check, Revision 5, performed on
Enclosure-22-NNS-ACB23 is one of the circuit breakers between preferred station serviceTransformer RTX-XSR1C and the Division III 4.16 kV ESF bus.Analysis: The performance deficiency associated with this finding involved thelicensee's failure to provide operators with an adequate STP to meet the requirements
              May 14 and 15, 2006
of TS SR 3.8.1.1 to verify correct breaker alignment and indicated power availability tothe Division III ESF bus for each required offsite circuit. A review of previous revisionsof STP-000-0102 showed that the procedure has never verified the required offsite
                                              -20-                                     Enclosure
power circuits for the Division III 4.16 kV ESF bus in Modes 1, 2, and 3. Although thisperformance deficiency caused the failure to verify the offsite power circuit for an
 
  *       STP-508-4543, Turbine First Stage Pressure Channel Functional Test,
            Revision 7, performed on June 4, 2006
  *       Reactor coolant sample using Procedures COP-0001, Sampling via Various
            Balance-Of-Plant Systems, Attachment 8, Reactor Sample Panel Routine
            Sample Points, Revision 14, and COP-0305, Operation of the Countroom
            Analysis Systems, Revision 2, performed on June 15, 2006
  Documents reviewed by the inspectors are listed in the attachment.
  The inspectors completed six inspection samples.
h. Findings
  Introduction: The inspectors identified an NCV of TS 5.4.1.a for the failure of the
  licensee to provide an adequate surveillance test procedure to perform TS Surveillance
  Requirement (SR) 3.8.1.1. Specifically, STP-000-0102, Power Distribution Alignment
  Check, Revision 4, did not include steps to verify the required offsite power circuit
  breaker alignment and indicated power availability for the Division III 4.16 kV ESF bus
  as required in Modes 1, 2, and 3.
  Description: As discussed in Section 1R15 of this report, operators failed to properly
  rack in Breaker NNS-ACB23 on April 29, 2006. This condition was discovered on
  May 22, when the breaker failed to close. During this period, on May 14, 2006, the
  Division I EDG was removed from service to replace a leaking section of jacket cooling
  water vent tubing. With the Division I EDG removed from service, TS Required
  Action 3.8.1.a.1 required that operators perform TS SR 3.8.1.1 within one hour and
  once every 8 hours until the EDG was operable. TS SR 3.8.1.1 required operators to
  verify the correct breaker alignment and indicated power for each required offsite power
  circuit. Operators utilized Procedure STP-000-0102, Power Distribution Alignment
  Check, Revision 4, to satisfy the requirements of TS SR 3.8.1.1; however, the
  inspectors identified that the procedure did not have steps to verify the correct breaker
  alignment and indicated power availability to the Division III 4.16 kV ESF bus. As a
  result, the operators did not identify that Breaker NNS-ACB23 was not racked in.
  During the period that the Division I EDG was removed from service, the plant was
  actually in TS Condition 3.8.1.d. TS Condition 3.8.1.d states that with One required
  offsite circuit inoperable AND one required [E]DG inoperable, restore the EDG or the
  offsite power supply to an operable status in 12 hours or place the plant in Mode 3 within
  the next 12 hours. The Division I EDG was inoperable for 15 hours and 15 minutes.
  Procedure STP-000-0102, Section 1.1, states, in part, that its purpose is to verify the
  correct breaker alignment and indicated power availability for each required offsite
  power circuit in accordance with TS SR 3.8.1.1 in Modes 1, 2, and 3. TS 3.8.1 bases
  defines an offsite power circuit as follows: Each offsite circuit consists of incoming
  breakers and disconnects to the respective preferred station service Transformers 1C
  and 1D [RSS1 and RSS2], the 1C and 1D preferred station service transformers, and
  the respective circuit path including feeder breakers to the three 4.16 kV ESF buses.
                                            -21-                                     Enclosure
 
NNS-ACB23 is one of the circuit breakers between preferred station service
Transformer RTX-XSR1C and the Division III 4.16 kV ESF bus.
Analysis: The performance deficiency associated with this finding involved the
licensees failure to provide operators with an adequate STP to meet the requirements
of TS SR 3.8.1.1 to verify correct breaker alignment and indicated power availability to
the Division III ESF bus for each required offsite circuit. A review of previous revisions
of STP-000-0102 showed that the procedure has never verified the required offsite
power circuits for the Division III 4.16 kV ESF bus in Modes 1, 2, and 3. Although this
performance deficiency caused the failure to verify the offsite power circuit for an
extended period of time, the risk impact was limited to the 10 days from May 12-22,
extended period of time, the risk impact was limited to the 10 days from May 12-22,
2006. Therefore, the risk characterization of this finding is the same as that described in
2006. Therefore, the risk characterization of this finding is the same as that described in
Section 1R15 of this inspection report. The cause of the finding was related to the
Section 1R15 of this inspection report. The cause of the finding was related to the
crosscutting aspect of human performance because the licensee did not provide the
crosscutting aspect of human performance because the licensee did not provide the
operators with an adequate STP to complete the TS SR to verify the required offsite
operators with an adequate STP to complete the TS SR to verify the required offsite
power circuits' breaker alignment to all three 4.16 kV ESF buses. Additionally, the
power circuits breaker alignment to all three 4.16 kV ESF buses. Additionally, the
cause of the finding was related to the cr
cause of the finding was related to the crosscutting aspect of problem identification and
osscutting aspect of problem identification andresolution in that on two occasions, June 18, 2005, and May 22, 2006, operatorsentered TS Condition 3.8.1.a for one inoperable offsite power circuit to the Division III
resolution in that on two occasions, June 18, 2005, and May 22, 2006, operators
entered TS Condition 3.8.1.a for one inoperable offsite power circuit to the Division III
4.16 kV ESF bus and performed STP-000-0102 to meet the Required Action to perform
4.16 kV ESF bus and performed STP-000-0102 to meet the Required Action to perform
SR 3.8.1.1, but did not recognize that STP-000-0102 did not verify the other offsitepower circuit breaker alignment to the Division III 4.16 kV ESF bus.Enforcement: TS 5.4.1.a requires that written procedures be established, implemented,and maintained covering the activities specified in Appendix A, "Typical Procedures for
SR 3.8.1.1, but did not recognize that STP-000-0102 did not verify the other offsite
Pressurized Water Reactors and Boiling Water Reactors," of Regulatory Guide 1.33,"Quality Assurance Program Requirements (Operation)," dated February 1978.  
power circuit breaker alignment to the Division III 4.16 kV ESF bus.
Regulatory Guide 1.33, Appendix A, Section 8.a, requires procedures for all TS SRs. Procedure STP-000-0102 states that it verified the correct breaker alignment and power
Enforcement: TS 5.4.1.a requires that written procedures be established, implemented,
availability for each required offsite circuit in accordance with TS SR 3.8.1.1 in Modes 1,2, and 3. Contrary to this, Procedure STP-000-0102, Revision 4, did not require
and maintained covering the activities specified in Appendix A, "Typical Procedures for
Pressurized Water Reactors and Boiling Water Reactors," of Regulatory Guide 1.33,
"Quality Assurance Program Requirements (Operation)," dated February 1978.
Regulatory Guide 1.33, Appendix A, Section 8.a, requires procedures for all TS SRs.
Procedure STP-000-0102 states that it verified the correct breaker alignment and power
availability for each required offsite circuit in accordance with TS SR 3.8.1.1 in Modes 1,
2, and 3. Contrary to this, Procedure STP-000-0102, Revision 4, did not require
verification of the correct breaker alignment for the offsite power circuits to the
verification of the correct breaker alignment for the offsite power circuits to the
Division III 4.16 kV ESF bus in Modes 1, 2, and 3. The root cause involved the incorrectinterpretation of the Division III 4.16 kV bus SRs as they apply to the unique River BendStation ESF electrical distribution system. The corrective actions to restore complianceincluded as an interim measure entering in the control room logs the breaker alignment
Division III 4.16 kV ESF bus in Modes 1, 2, and 3. The root cause involved the incorrect
for and the bus voltage available to the Division III 4.16 kV ESF bus, until STP-000-0102could be revised. Because the finding was of very low safety significance and has been
interpretation of the Division III 4.16 kV bus SRs as they apply to the unique River Bend
entered into the licensee's CAP as CR-RBS-2006-02675 and -02402, this violation is
Station ESF electrical distribution system. The corrective actions to restore compliance
being treated as an NCV consistent with Section VI.A of the Enforcement Policy: NCV
included as an interim measure entering in the control room logs the breaker alignment
05000458/2006003-03, "Inadequate procedure to verify required offsite power breaker
for and the bus voltage available to the Division III 4.16 kV ESF bus, until STP-000-0102
alignment."
could be revised. Because the finding was of very low safety significance and has been
Enclosure-23-1R23Temporary Plant Modifications     a.Inspection ScopeThe inspectors reviewed the USAR, plant drawings, procedure requirements, and TS toensure that Temporary Alteration 2006-0011, Off Gas Pretreatment Radiation MonitorSample Chamber Drain Line Modification, was properly implemented. The inspectors:  
entered into the licensees CAP as CR-RBS-2006-02675 and -02402, this violation is
(1) verified that the modification did not have an affe
being treated as an NCV consistent with Section VI.A of the Enforcement Policy: NCV
ct on system operability/availability;(2) verified that the installation was consistent with modification documents; (3) ensured
05000458/2006003-03, Inadequate procedure to verify required offsite power breaker
that the postinstallation test results were satisfactory and that the impact of the
alignment.
temporary modification on the operation of the pretreatment radiation monitor weresupported by the test; (4) verified that the modification was identified on control roomdrawings and that appropriate identification tags were placed on the affected drawings;and (5) verified that appropriate safety evaluations were completed. The inspectors
                                          -22-                                     Enclosure
verified that the licensee identified and implemented any needed corrective actions
 
associated with temporary modifications.The inspectors completed one inspection sample.   b.FindingsNo findings of significance were identified.
1R23 Temporary Plant Modifications
Cornerstone: Emergency Preparedness1EP6Drill Evaluation     a.Inspection ScopeOn June 20, 2006, the inspectors observed the full scope exercise dress rehearsal,which was used to contribute to "Drill/Exercise Performance" and "Emergency ResponseOrganization Drill Performance" PI. The inspectors: (1) observed the training evolutionto identify any weaknesses and deficiencies in classification, notification, and protective
  a. Inspection Scope
action requirements development activities; (2) compared the identified weaknesses and
      The inspectors reviewed the USAR, plant drawings, procedure requirements, and TS to
deficiencies against licensee identified findings to determine whether the licensee was
      ensure that Temporary Alteration 2006-0011, Off Gas Pretreatment Radiation Monitor
properly identifying failures; and (3) determined whether licensee performance was in
      Sample Chamber Drain Line Modification, was properly implemented. The inspectors:
accordance with the guidance of the NEI 99-02, "Voluntary Submission of Performance
      (1) verified that the modification did not have an affect on system operability/availability;
Indicator Data," Revision 2, acceptance criteria. The scenario used was RDRL-EP-0602, Tornado/Loss of Offsite Power/Main Steam Line Break, dated June 16, 2006.Emergency [plan] implementing procedures reviewed by the inspectors included:
      (2) verified that the installation was consistent with modification documents; (3) ensured
*EIP-2-001, "Classification of Emergencies," Revision 13*EIP-2-006, "Notifications," Revision 32
      that the postinstallation test results were satisfactory and that the impact of the
*EIP-2-007, "Protective Action Guidelines Recommendations," Revision 21The inspectors completed one inspection sample.  
      temporary modification on the operation of the pretreatment radiation monitor were
Enclosure-24-     b.FindingsNo findings of significance were identified.2.RADIATION SAFETYCornerstone: Occupational Radiation Safety2OS1Access Control to Radiologically Significant Areas     a.Inspection ScopeThis area was inspected to assess the licensee's performance in implementing physicaland administrative controls for airborne radioactivity areas, radiation areas, high
      supported by the test; (4) verified that the modification was identified on control room
radiation areas, and worker adherence to these controls. The inspector used the
      drawings and that appropriate identification tags were placed on the affected drawings;
requirements in 10 CFR Part 20, TS, and the licensee's procedures required by TS as
      and (5) verified that appropriate safety evaluations were completed. The inspectors
criteria for determining compliance. During the inspection, the inspector interviewed the
      verified that the licensee identified and implemented any needed corrective actions
radiation protection manager, radiation protection supervisors, and radiation workers.  
      associated with temporary modifications.
The inspector performed independent radiation dose rate measurements and reviewed
      The inspectors completed one inspection sample.
the following items:*PI events and associated documentation packages reported by the licensee inthe occupational radiation safety cornerstone*Controls (surveys, posting, and barricades) of three radiation, high radiation, orairborne radioactivity areas*Radiation work permits, procedures, engineering controls, and air samplerlocations *Conformation of electronic personal dosimeter alarm setpoints with surveyindications and plant policy; workers' knowledge of required actions when their
  b. Findings
electronic personnel dosimeter noticeably malfunctions or alarms*Barrier integrity and performance of engineering controls in airborne radioactivityareas*Adequacy of the licensee's internal dose assessment for any actual internalexposure greater than 50 millirem committed effective dose equivalent*Physical and programmatic controls for highly activated or contaminatedmaterials (nonfuel) stored within spent fuel and other storage pools. *Self-assessments, audits, licensee event reports (LER), and special reportsrelated to the access control program since the last inspection *Corrective action documents related to access controls
      No findings of significance were identified.
Enclosure-25-*Licensee actions in cases of repetitive deficiencies or significant individualdeficiencies  *Radiation work permit briefings and worker instructions  
      Cornerstone: Emergency Preparedness
*Adequacy of radiological controls, such as required surveys, radiation protectionjob coverage, and contamination controls during job performance *Dosimetry placement in high radiation work areas with significant dose rategradients *Changes in licensee procedural controls of high dose rate - high radiation areasand very high radiation areas*Controls for special areas that have the potential to become very high radiationareas during certain plant operations*Posting and locking of entrances to all accessible high dose rate - high radiationareas and very high radiation areas *Radiation worker and radiation protection technician performance with respect toradiation protection work requirements The inspector completed 21 of the required 21 samples.     b.Findings   1.Unguarded High Radiation Area BoundaryIntroduction: The inspector reviewed a self-revealing NCV of TS 5.7.1, resulting fromthe licensee's failure to control access to a high radiation area. The finding had very low
1EP6 Drill Evaluation
safety significance.Description: On April 6, 2006, the licensee transferred reverse osmosis system filtersfrom one elevation of the radwaste building to another. Because dose rates on the filter
  a. Inspection Scope
barrels were as high as 600 millirem per hour, the licensee assigned personnel to guardthe elevator entrances to prevent workers from entering high radiation areas. On this
      On June 20, 2006, the inspectors observed the full scope exercise dress rehearsal,
occasion, the guards were not using radios, as was a common practice. Because of the
      which was used to contribute to Drill/Exercise Performance and Emergency Response
lack of good communication, a guard prematurely left his post in front of the 123-foot
      Organization Drill Performance PI. The inspectors: (1) observed the training evolution
elevation elevator door. Coincidently, two workers attempted to board the elevator on
      to identify any weaknesses and deficiencies in classification, notification, and protective
the 123-foot elevation after the guard had left. The elevator carrying the barrels ofradioactive filters stopped at the 123-foot elevation, the doors opened, and theelectronic dosimeters of the workers alarmed because of the high dose rates. The
      action requirements development activities; (2) compared the identified weaknesses and
guard returned and evacuated the workers before they accrued additional radiation
      deficiencies against licensee identified findings to determine whether the licensee was
dose. The highest dose rate recorded by an electronic alarming dosimeter was 164
      properly identifying failures; and (3) determined whether licensee performance was in
millirem per hour. Planned corrective action was still being evaluated by the licensee atthe conclusion of the inspection.  
      accordance with the guidance of the NEI 99-02, "Voluntary Submission of Performance
Enclosure-26-Analysis: The failure to control access to a high radiation area was a performancedeficiency.  The significance of the finding was greater than minor because it was
      Indicator Data," Revision 2, acceptance criteria. The scenario used was RDRL-EP-
associated with the occupational radiation safety attribute of exposure control and
      0602, Tornado/Loss of Offsite Power/Main Steam Line Break, dated June 16, 2006.
affected the cornerstone objective, in that not controlling access to a high radiation areacould increase personal exposure. Using the Occupational Radiation Safety
      Emergency [plan] implementing procedures reviewed by the inspectors included:
Significance Determination Process, the inspector determined that the finding was ofvery low safety significance because it did not involve: (1) an as low as is reasonably
      *       EIP-2-001, Classification of Emergencies, Revision 13
achievable (ALARA) finding, (2) an overexposure, (3) a substantial potential foroverexposure, or (4) an impaired ability to assess dose. Additionally, this finding hadcrosscutting aspects associated with human performance in that the failure of the
      *       EIP-2-006, Notifications, Revision 32
individual to guard the elevator door directly contributed to the violation.Enforcement: TS 5.7.1 requires each high radiation area, as defined in 10 CFR Part 20,in which the intensity of radiation is greater than 100 millirems per hour but less than1000 millirems per hour, be barricaded and conspicuously posted as a high radiationarea and entrance thereto shall be controlled by requiring issuance of a radiation work
      *       EIP-2-007, Protective Action Guidelines Recommendations, Revision 21
permit. The licensee violated TS 5.7.1 when it failed to barricade and conspicuously
      The inspectors completed one inspection sample.
post the elevator housing the radioactive filter barrels or maintain a guard to ensure
                                              -23-                                     Enclosure
workers did not enter a high radiation area. Because this failure to control a high
 
radiation area was of very low safety significance and has been entered into the
  b. Findings
licensee's CAP as CR-RBS-2006-01294, this violation is being treated as an NCV,
      No findings of significance were identified.
consistent with Section VI.A of the NRC Enforcement Policy:  
2.   RADIATION SAFETY
NCV 05000458/2006003-04, "Failure to control access to a high radiation area."    2.Unanalyzed Airborne Radioactivity SurveyIntroduction: The inspector identified an NCV of 10 CFR 20.1501(a) because thelicensee failed to survey airborne radioactivity. The finding had very low significance.Description: On May 2, 2006, during the removal of local power range monitors, thelicensee started collecting an air sample of the work area. The air sample spanned two
      Cornerstone: Occupational Radiation Safety
shifts. A health physics technician on the second shift discarded the sample because
2OS1 Access Control to Radiologically Significant Areas
the first shift had not documented a start time. Therefore, the sample was never
  a. Inspection Scope
analyzed. However, all workers successfully passed through the portal monitors at the
      This area was inspected to assess the licensees performance in implementing physical
exit of the controlled access area without alarm, confirming that no worker experienced
      and administrative controls for airborne radioactivity areas, radiation areas, high
an uptake of radioactive material. Planned corrective action is still being evaluated.Analysis: The failure to survey airborne radioactivity was a performance deficiency. This finding was greater than minor because it was associated with the occupational
      radiation areas, and worker adherence to these controls. The inspector used the
radiation safety program attribute of exposure control and affected the cornerstone
      requirements in 10 CFR Part 20, TS, and the licensees procedures required by TS as
objective in that the lack of knowledge of radiological conditions could increase
      criteria for determining compliance. During the inspection, the inspector interviewed the
personnel dose. Using the Occupational Radiation Safety Significance Determination
      radiation protection manager, radiation protection supervisors, and radiation workers.
Process, the inspector determined that the finding was of very low safety significance
      The inspector performed independent radiation dose rate measurements and reviewed
because it did not involve: (1) an ALARA finding, (2) an overexposure, (3) a substantial
      the following items:
potential for overexposure, or (4) an impaired ability to assess dose.   Additionally, thisfinding had crosscutting aspects associated with human performance in that the failureto maintain the sample for analysis directly contributed to the violation.  
      *       PI events and associated documentation packages reported by the licensee in
Enclosure-27-Enforcement: 10 CFR 20.1501(a) requires that each licensee make or cause to bemade surveys that may be necessary for the licensee to comply with the regulations in
              the occupational radiation safety cornerstone
10 CFR Part 20 and that are reasonable under the circumstances to evaluate the extentof radiation levels, concentrations or quantities of radioactive materials, and the potential
      *       Controls (surveys, posting, and barricades) of three radiation, high radiation, or
radiological hazards that could be present. Pursuant to 10 CFR 20.1003, a "survey"
              airborne radioactivity areas
means an evaluation of the radiological conditions and potential hazards incident to the
      *       Radiation work permits, procedures, engineering controls, and air sampler
production, use, transfer, release, disposal, or presence of radioactive material or other
              locations
sources of radiation. In part, 10 CFR 20.1201(a) states that the licensee shall controlthe occupational dose to individual adults. The licensee violated 10 CFR 20.1501(a)
      *       Conformation of electronic personal dosimeter alarm setpoints with survey
when it failed to perform an evaluation of airborne radioactivity to ensure compliance
              indications and plant policy; workers knowledge of required actions when their
with 10 CFR 20.1201(a). Because this failure to perform a radiological survey was of
              electronic personnel dosimeter noticeably malfunctions or alarms
very low safety significance and has been entered into the licensee's CAP as
      *       Barrier integrity and performance of engineering controls in airborne radioactivity
CR-RBS-2006-01994, this violation is being treated as an NCV, consistent with
              areas
Section VI.A of the NRC Enforcement Policy: NCV 05000458/2006003-05, "Failure toperform airborne radiation survey."2OS2ALARA Planning and Controls     a.Inspection ScopeThe inspector assessed licensee performance with respect to maintaining individual andcollective radiation exposures ALARA. The inspector used the requirements in 10 CFR
      *       Adequacy of the licensees internal dose assessment for any actual internal
Part 20 and the licensee's procedures required by TS as criteria for determining
              exposure greater than 50 millirem committed effective dose equivalent
compliance. The inspector interviewed licensee personnel and reviewed:*Current 3-year rolling average collective exposure  
      *       Physical and programmatic controls for highly activated or contaminated
*Three outage or on-line maintenance work activities scheduled during theinspection period and associated work activity exposure estimates which were
              materials (nonfuel) stored within spent fuel and other storage pools.
likely to result in the highest personnel collective exposures *ALARA work activity evaluations, exposure estimates, and exposure mitigationrequirements*Intended versus actual work activity doses and the reasons for anyinconsistencies *Shielding requests and dose/benefit analyses
      *       Self-assessments, audits, licensee event reports (LER), and special reports
*Dose rate reduction activities in work planning  
              related to the access control program since the last inspection
*Use of engineering controls to achieve dose reductions and dose reductionbenefits afforded by shielding *Workers use of the low dose waiting areas
      *       Corrective action documents related to access controls
*First-line job supervisors' contribution to ensuring work activities are conductedin a dose efficient manner
                                              -24-                                   Enclosure
Enclosure-28-*Radiation worker and radiation protection technician performance during workactivities in radiation areas, airborne radioactivity areas, or high radiation areas The inspector completed 6 of the required 15 samples and 4 of the optional samples.     b.FindingsNo findings of significance were identified.4.OTHER ACTIVITIES
 
4OA1Performance Indicator Verification    a.Inspection Scope    1.Barrier Integrity CornerstoneThe inspectors sampled licensee submittals for the two PIs listed below for the periodOctober 1, 2004, through March 31, 2006. The definitions and guidance of NEI 99-02,
    *       Licensee actions in cases of repetitive deficiencies or significant individual
"Regulatory Assessment Indicator Guideline," Revision 4, were used to verify the
            deficiencies
licensee's basis for reporting each data element in order to verify the accuracy of PI
    *       Radiation work permit briefings and worker instructions
data reported during the assessment period. The inspectors: (1) reviewed reactor
    *       Adequacy of radiological controls, such as required surveys, radiation protection
coolant system (RCS) chemistry sample analyses for dose equivalent Iodine-131 andcompared the results to the TS limit; (2) observed a chemistry technician obtain and
            job coverage, and contamination controls during job performance
analyze an RCS sample; (3) reviewed operating logs and surveillance results formeasurements of RCS identified leakage; and (4) observed a surveillance test thatdetermined RCS identified leakage.RCS Specific ActivityRCS LeakageThe inspectors completed two inspection samples.    2.Occupational Radiation Safety CornerstoneThe review included corrective action documentation that identified occurrences inlocked high radiation areas (as defined in the licensee's TS), very high radiation areas
    *       Dosimetry placement in high radiation work areas with significant dose rate
(as defined in 10 CFR 20.1003), and unplanned personnel exposures (as defined in
            gradients
NEI 99-02), specifically CR-RBS-2006-01910. Additional records reviewed included
    *      Changes in licensee procedural controls of high dose rate - high radiation areas
ALARA records and whole-body counts of selected individual exposures. The inspector
            and very high radiation areas
interviewed licensee personnel that were accountable for collecting and evaluating the
    *       Controls for special areas that have the potential to become very high radiation
PI data. In addition, the inspector toured plant areas to verify that high radiation, lockedhigh radiation, and very high radiation areas were properly controlled. PI definitions and
            areas during certain plant operations
guidance contained in NEI 99-02, "Regulatory Assessment Indicator Guideline,"
    *       Posting and locking of entrances to all accessible high dose rate - high radiation
Revision 3, were used to verify the basis in reporting for each data element.  
            areas and very high radiation areas
Enclosure-29-*Occupational Exposure Control EffectivenessThe inspector completed the one required sample in this cornerstone.   3.Public Radiation Safety CornerstoneThe inspector reviewed licensee documents from June 1, 2005, through March 31,2006. Licensee records reviewed included corrective action documentation that
    *       Radiation worker and radiation protection technician performance with respect to
identified occurrences for liquid or gaseous effluent releases that exceeded PI
            radiation protection work requirements
thresholds and those reported to the NRC. The inspector interviewed licenseepersonnel that were accountable for collecting and evaluating the PI data. PI definitionsand guidance contained in NEI 99-02, "Regulatory Assessment Indicator Guideline,"
    The inspector completed 21 of the required 21 samples.
Revision 3, were used to verify the basis in reporting for each data element.*Radiological Effluent Technical Specification/Offsite Dose Calculation Manual Radiological Effluent Occurrences The inspector completed the one required sample in this cornerstone.     f.FindingsNo findings of significance were identified.4OA2Identification and Resolution of Problems   1.Semiannual Trend Review     g.Inspection ScopeThe inspectors completed a semiannual trend review of repetitive or closely relatedissues related to identify trends that might indicate the existence of more safety
b. Findings
significant issues. The inspectors' review consisted of the 6-month period from
1. Unguarded High Radiation Area Boundary
January 1 to June 30, 2006, of CAP items associated with the three EDG starting air
    Introduction: The inspector reviewed a self-revealing NCV of TS 5.7.1, resulting from
systems documented in 42 CRs. When warranted, some of the samples expandedbeyond those dates to fully assess the issue. The inspectors compared and contrasted
    the licensees failure to control access to a high radiation area. The finding had very low
their results with the results contained in adverse trend CRs for problems related to the
    safety significance.
starting air compressors and air dryers. Corrective actions associated with a sample of
    Description: On April 6, 2006, the licensee transferred reverse osmosis system filters
the issues identified were reviewed for adequacy. The CRs reviewed by the inspectors
    from one elevation of the radwaste building to another. Because dose rates on the filter
are listed in the attachment.The inspectors completed one inspection sample.     b. Findings and ObservationsThere were no findings of significance identified associated with the CRs reviewed.
    barrels were as high as 600 millirem per hour, the licensee assigned personnel to guard
The inspectors noted that the licensee had identified a long-standing issue related to theperformance of the EDG starting air systems' air compressors. Since January 1, 2006,  
    the elevator entrances to prevent workers from entering high radiation areas. On this
Enclosure-30-there were 18 CRs written for high metal wear products in monthly air compressor oilsamples. Each of these CRs was closed to CR-RBS-2004-02165. An additional
    occasion, the guards were not using radios, as was a common practice. Because of the
28 CRs written since August 2, 2004, for high metal wear product concentrations and
    lack of good communication, a guard prematurely left his post in front of the 123-foot
high moisture content in monthly compressor oil samples were closed to CR-RBS-2004-
    elevation elevator door. Coincidently, two workers attempted to board the elevator on
02165. In addition, operators wrote adverse trend CR-RBS-2006-02407 to detail
    the 123-foot elevation after the guard had left. The elevator carrying the barrels of
compressor problems, including excessive run times. The inspectors determined that
    radioactive filters stopped at the 123-foot elevation, the doors opened, and the
the licensee is taking appropriate actions to understand the problem with the EDG
    electronic dosimeters of the workers alarmed because of the high dose rates. The
starting air compressors, including sending  
    guard returned and evacuated the workers before they accrued additional radiation
the system engineer to observe the vendor'steardown and refurbishment of two of the starting air compressors. Another four CRs have been written since January 1, 2006, describing problems withstarting air system dryers and dryer prefilters. Following a June 29, 2006, meeting heldto discuss overall EDG starting air system maintenance problems, the licensee wroteCR-RBS-2006-02799, to look into the relationship between the prefilter and dryer
    dose. The highest dose rate recorded by an electronic alarming dosimeter was 164
problems. The inspectors noted that this meeting was the first discussion of the overall
    millirem per hour. Planned corrective action was still being evaluated by the licensee at
condition of the EDG starting air systems and to evaluate the interrelationship betweencompressor, dryer, and prefilter problems. 2.Occupational Radiation Safety     a.Inspection ScopeThe inspector evaluated the effectiveness of the licensee's problem identification andresolution process with respect to the following inspection areas:*Access Control to Radiologically Significant Areas (Section 2OS1)*ALARA Planning and Controls (Section 2OS2)     b. Findings and ObservationsNo findings of significance were identified. 3.Inservice Inspection Activities     a.Inspection ScopeThe inspector reviewed selected inservice inspection related CRs issued during thecurrent and past refueling outages. The review served to verify that the licensee's CAP
    the conclusion of the inspection.
was being correctly utilized to identify conditions adverse to quality and that thoseconditions were being adequately evaluated, corrected, and trended.     b.FindingsNo findings of significance were identified.  
                                            -25-                                       Enclosure
Enclosure-31-4OA3Event Followup   1.(Closed) LER 50-458/2004-003-01, Unplanned Automatic Start of Standby DieselGenerator Due to Loss of Division 1 Switchgear On October 31, 2004, technicians caused an unexpected degraded voltage signal,which resulted in a loss of the Division I 4.16 kV ESF bus during preparations for the
 
Division I loss of offsite power/loss of coolant accident test. The Division I EDG
  Analysis: The failure to control access to a high radiation area was a performance
automatically started and powered the ESF bus and all equipment operated asexpected. Initial inspection of this event was documented in NRC integrated inspection
  deficiency. The significance of the finding was greater than minor because it was
Report 05000458/2004005. During this inspection period, the inspectors reviewed the
  associated with the occupational radiation safety attribute of exposure control and
LER, the root cause analysis, and corrective actions documented in
  affected the cornerstone objective, in that not controlling access to a high radiation area
CR-RBS-2004-03518. No additional findings of significance were identified. This LER
  could increase personal exposure. Using the Occupational Radiation Safety
is closed.   2.(Closed) LER 50-458/2004-004-01, Unplanned Automatic Start of Standby DieselGenerator Due to Loss of Division 2 SwitchgearOn November 1, 2004, technicians inadvertently caused a trip of Transformer RSS2preferred station service Transformer RTX-XSR1F while troubleshooting a transformer
  Significance Determination Process, the inspector determined that the finding was of
sudden pressure relay trip circuit. As a result, power was also lost to preferred station
  very low safety significance because it did not involve: (1) an as low as is reasonably
Transformer RTX-XSR1D and the Division II 4.16 kV ESF bus. The running shutdown
  achievable (ALARA) finding, (2) an overexposure, (3) a substantial potential for
cooling, alternate decay heat removal, and plant operating water cleanup systems lostpower until the Division II EDG started and restored power to the ESF bus. Shutdown
  overexposure, or (4) an impaired ability to assess dose. Additionally, this finding had
cooling was restored in less than one hour. Initial inspection of this event was
  crosscutting aspects associated with human performance in that the failure of the
documented in NRC integrated inspection Report 05000458/2004005. During thisinspection period, the inspectors reviewed the LER, the root cause analysis, and
  individual to guard the elevator door directly contributed to the violation.
corrective actions documented in CR-RBS-2004-03546. No additional findings of
  Enforcement: TS 5.7.1 requires each high radiation area, as defined in 10 CFR Part 20,
significance were identified. This LER is closed.   3.(Closed) LER 50-458/2004-005-01, Unplanned Automatic Scram Due to Loss ofNon-Vital 120 Volt Instrument BusOn December 10, 2004, an automatic scram occurred due to a loss of power tononsafety-related instrumentation Bus VBN-PNL01B1. A capacitor on the control boardfor the nonsafety-related Inverter BYS-INV01B static switch failed, which caused a loss
  in which the intensity of radiation is greater than 100 millirems per hour but less than
of power to Bus VBN-PNL01B1, a subsequent downshift of the plant operating
  1000 millirems per hour, be barricaded and conspicuously posted as a high radiation
recirculation pumps and a lockup of the main feedwater regulating valves. The result
  area and entrance thereto shall be controlled by requiring issuance of a radiation work
was an automatic plant scram complicated by a loss of normal feedwater. Inspection of
  permit. The licensee violated TS 5.7.1 when it failed to barricade and conspicuously
this event was documented in NRC integrated inspection Report 05000458/2004005. Additional inspection was documented in  
  post the elevator housing the radioactive filter barrels or maintain a guard to ensure
NRC supplemental inspection Report05000458/2005012. During this inspection period, the inspectors reviewed the LER, the
  workers did not enter a high radiation area. Because this failure to control a high
root cause analysis, and corrective actions documented in CR-RBS-2004-04289. No
  radiation area was of very low safety significance and has been entered into the
additional findings of significance were identified. This LER is closed.  
  licensees CAP as CR-RBS-2006-01294, this violation is being treated as an NCV,
Enclosure-32-   4.(Closed) LER 50-458 /2005-001-01, Unplanned Manual Scram Due to Indication ofGround Fault in Main GeneratorOn January 15, 2005, while the plant was at 100 percent power, a main generator fieldground fault alarm was received. Control room operators tripped the turbine in
  consistent with Section VI.A of the NRC Enforcement Policy:
accordance with alarm response Procedure ARP-680-09. The licensee later determined
  NCV 05000458/2006003-04, Failure to control access to a high radiation area.
that one of the five rectifier banks in the generator excitation control system was thesource of the ground and removed it from service. In addition, the licensee tested the
2. Unanalyzed Airborne Radioactivity Survey
relay that causes the main generator ground fault alarm and found it to be out of
  Introduction: The inspector identified an NCV of 10 CFR 20.1501(a) because the
calibration such that it alarmed before the ground current reached its setpoint. The
  licensee failed to survey airborne radioactivity. The finding had very low significance.
alarm response procedure requirement to trip the turbine was revised to allow validation
  Description: On May 2, 2006, during the removal of local power range monitors, the
of the alarm before tripping the main turbine. Inspection of this event was documented
  licensee started collecting an air sample of the work area. The air sample spanned two
in NRC integrated inspection Report 05000458/2005002. Additional inspection wasdocumented in NRC supplemental inspection Report 05000458/2005012. During thisinspection period, the inspectors reviewed the LER, the root cause analysis, and
  shifts. A health physics technician on the second shift discarded the sample because
corrective actions documented in CR-RBS-2005-00140. No additional findings of
  the first shift had not documented a start time. Therefore, the sample was never
significance were identified. This LER is closed.4OA5Other ActivitiesImplementation of Temporary Instruction 2515/165 - Operational Readiness of OffsitePower and Impact on Plant Risk     a.Inspection ScopeThe objective of Temporary Instruction 2515/165, "Operational Readiness of OffsitePower and Impact on Plant Risk," was to gather information to support the assessment
  analyzed. However, all workers successfully passed through the portal monitors at the
of nuclear power plant operational readiness of offsite power systems and impact onplant risk. During this inspection, the inspectors interviewed licensee personnel,
  exit of the controlled access area without alarm, confirming that no worker experienced
reviewed licensee procedures, and gathered information for further evaluation by the
  an uptake of radioactive material. Planned corrective action is still being evaluated.
Office of Nuclear Reactor Regulation.       b.FindingsNo findings of significance were identified.4OA6Meetings, Including ExitExit MeetingsOn May 5, 2006, the inspector presented the occupational radiation safety inspectionresults to Mr. D. Vinci, General Manager, Plant Operations, and other members of his
  Analysis: The failure to survey airborne radioactivity was a performance deficiency.
staff who acknowledged the findings. The inspector confirmed that proprietary
  This finding was greater than minor because it was associated with the occupational
information was not provided or examined during the inspection.On May 5, 2006, the inspector presented the results of this inspection of inserviceinspection activities to Mr. P. Russell, Manager, System Engineering, and other  
  radiation safety program attribute of exposure control and affected the cornerstone
Enclosure-33-members of licensee management. The inspector confirmed that proprietaryinformation was not provided or examined during the inspection.On July 5, 2006, the resident inspectors presented the integrated baseline inspectionresults to Mr. P. Hinnenkamp, Vice President - Operations, and other members of
  objective in that the lack of knowledge of radiological conditions could increase
licensee management. The inspectors confirmed that proprietary information was not
  personnel dose. Using the Occupational Radiation Safety Significance Determination
provided or examined during the inspection.ATTACHMENT: SUPPLEMENTAL INFORMATION  
  Process, the inspector determined that the finding was of very low safety significance
AttachmentA-1SUPPLEMENTAL INFORMATIONKEY POINTS OF CONTACTLicensee PersonnelT. Baccus, Acting Supervisor, ALARA PlanningL. Ballard, Manager, Quality Programs
  because it did not involve: (1) an ALARA finding, (2) an overexposure, (3) a substantial
  potential for overexposure, or (4) an impaired ability to assess dose. Additionally, this
  finding had crosscutting aspects associated with human performance in that the failure
  to maintain the sample for analysis directly contributed to the violation.
                                            -26-                                     Enclosure
 
    Enforcement: 10 CFR 20.1501(a) requires that each licensee make or cause to be
    made surveys that may be necessary for the licensee to comply with the regulations in
    10 CFR Part 20 and that are reasonable under the circumstances to evaluate the extent
    of radiation levels, concentrations or quantities of radioactive materials, and the potential
    radiological hazards that could be present. Pursuant to 10 CFR 20.1003, a survey
    means an evaluation of the radiological conditions and potential hazards incident to the
    production, use, transfer, release, disposal, or presence of radioactive material or other
    sources of radiation. In part, 10 CFR 20.1201(a) states that the licensee shall control
    the occupational dose to individual adults. The licensee violated 10 CFR 20.1501(a)
    when it failed to perform an evaluation of airborne radioactivity to ensure compliance
    with 10 CFR 20.1201(a). Because this failure to perform a radiological survey was of
    very low safety significance and has been entered into the licensees CAP as
    CR-RBS-2006-01994, this violation is being treated as an NCV, consistent with
    Section VI.A of the NRC Enforcement Policy: NCV 05000458/2006003-05, Failure to
    perform airborne radiation survey.
2OS2 ALARA Planning and Controls
  a. Inspection Scope
    The inspector assessed licensee performance with respect to maintaining individual and
    collective radiation exposures ALARA. The inspector used the requirements in 10 CFR
    Part 20 and the licensees procedures required by TS as criteria for determining
    compliance. The inspector interviewed licensee personnel and reviewed:
    *       Current 3-year rolling average collective exposure
    *       Three outage or on-line maintenance work activities scheduled during the
            inspection period and associated work activity exposure estimates which were
            likely to result in the highest personnel collective exposures
    *       ALARA work activity evaluations, exposure estimates, and exposure mitigation
            requirements
    *       Intended versus actual work activity doses and the reasons for any
            inconsistencies
    *       Shielding requests and dose/benefit analyses
    *       Dose rate reduction activities in work planning
    *       Use of engineering controls to achieve dose reductions and dose reduction
            benefits afforded by shielding
    *       Workers use of the low dose waiting areas
    *       First-line job supervisors contribution to ensuring work activities are conducted
            in a dose efficient manner
                                              -27-                                     Enclosure
 
      *       Radiation worker and radiation protection technician performance during work
              activities in radiation areas, airborne radioactivity areas, or high radiation areas
      The inspector completed 6 of the required 15 samples and 4 of the optional samples.
    b. Findings
      No findings of significance were identified.
4.     OTHER ACTIVITIES
4OA1 Performance Indicator Verification
     a. Inspection Scope
   1. Barrier Integrity Cornerstone
      The inspectors sampled licensee submittals for the two PIs listed below for the period
      October 1, 2004, through March 31, 2006. The definitions and guidance of NEI 99-02,
      Regulatory Assessment Indicator Guideline, Revision 4, were used to verify the
      licensees basis for reporting each data element in order to verify the accuracy of PI
      data reported during the assessment period. The inspectors: (1) reviewed reactor
      coolant system (RCS) chemistry sample analyses for dose equivalent Iodine-131 and
      compared the results to the TS limit; (2) observed a chemistry technician obtain and
      analyze an RCS sample; (3) reviewed operating logs and surveillance results for
      measurements of RCS identified leakage; and (4) observed a surveillance test that
      determined RCS identified leakage.
      C      RCS Specific Activity
      C      RCS Leakage
      The inspectors completed two inspection samples.
   2. Occupational Radiation Safety Cornerstone
      The review included corrective action documentation that identified occurrences in
      locked high radiation areas (as defined in the licensees TS), very high radiation areas
      (as defined in 10 CFR 20.1003), and unplanned personnel exposures (as defined in
      NEI 99-02), specifically CR-RBS-2006-01910. Additional records reviewed included
      ALARA records and whole-body counts of selected individual exposures. The inspector
      interviewed licensee personnel that were accountable for collecting and evaluating the
      PI data. In addition, the inspector toured plant areas to verify that high radiation, locked
      high radiation, and very high radiation areas were properly controlled. PI definitions and
      guidance contained in NEI 99-02, "Regulatory Assessment Indicator Guideline,"
      Revision 3, were used to verify the basis in reporting for each data element.
                                                -28-                                     Enclosure
 
      *       Occupational Exposure Control Effectiveness
      The inspector completed the one required sample in this cornerstone.
  3. Public Radiation Safety Cornerstone
      The inspector reviewed licensee documents from June 1, 2005, through March 31,
      2006. Licensee records reviewed included corrective action documentation that
      identified occurrences for liquid or gaseous effluent releases that exceeded PI
      thresholds and those reported to the NRC. The inspector interviewed licensee
      personnel that were accountable for collecting and evaluating the PI data. PI definitions
      and guidance contained in NEI 99-02, "Regulatory Assessment Indicator Guideline,"
      Revision 3, were used to verify the basis in reporting for each data element.
      *       Radiological Effluent Technical Specification/Offsite Dose Calculation Manual
              Radiological Effluent Occurrences
      The inspector completed the one required sample in this cornerstone.
  f. Findings
      No findings of significance were identified.
4OA2 Identification and Resolution of Problems
1.   Semiannual Trend Review
  g. Inspection Scope
      The inspectors completed a semiannual trend review of repetitive or closely related
      issues related to identify trends that might indicate the existence of more safety
      significant issues. The inspectors review consisted of the 6-month period from
      January 1 to June 30, 2006, of CAP items associated with the three EDG starting air
      systems documented in 42 CRs. When warranted, some of the samples expanded
      beyond those dates to fully assess the issue. The inspectors compared and contrasted
      their results with the results contained in adverse trend CRs for problems related to the
      starting air compressors and air dryers. Corrective actions associated with a sample of
      the issues identified were reviewed for adequacy. The CRs reviewed by the inspectors
      are listed in the attachment.
      The inspectors completed one inspection sample.
  b. Findings and Observations
      There were no findings of significance identified associated with the CRs reviewed.
      The inspectors noted that the licensee had identified a long-standing issue related to the
      performance of the EDG starting air systems air compressors. Since January 1, 2006,
                                              -29-                                   Enclosure
 
      there were 18 CRs written for high metal wear products in monthly air compressor oil
      samples. Each of these CRs was closed to CR-RBS-2004-02165. An additional
      28 CRs written since August 2, 2004, for high metal wear product concentrations and
      high moisture content in monthly compressor oil samples were closed to CR-RBS-2004-
      02165. In addition, operators wrote adverse trend CR-RBS-2006-02407 to detail
      compressor problems, including excessive run times. The inspectors determined that
      the licensee is taking appropriate actions to understand the problem with the EDG
      starting air compressors, including sending the system engineer to observe the vendors
      teardown and refurbishment of two of the starting air compressors.
      Another four CRs have been written since January 1, 2006, describing problems with
      starting air system dryers and dryer prefilters. Following a June 29, 2006, meeting held
      to discuss overall EDG starting air system maintenance problems, the licensee wrote
      CR-RBS-2006-02799, to look into the relationship between the prefilter and dryer
      problems. The inspectors noted that this meeting was the first discussion of the overall
      condition of the EDG starting air systems and to evaluate the interrelationship between
      compressor, dryer, and prefilter problems.
2.   Occupational Radiation Safety
  a. Inspection Scope
      The inspector evaluated the effectiveness of the licensees problem identification and
      resolution process with respect to the following inspection areas:
      *       Access Control to Radiologically Significant Areas (Section 2OS1)
      *       ALARA Planning and Controls (Section 2OS2)
  b. Findings and Observations
      No findings of significance were identified.
3.   Inservice Inspection Activities
  a. Inspection Scope
      The inspector reviewed selected inservice inspection related CRs issued during the
      current and past refueling outages. The review served to verify that the licensees CAP
      was being correctly utilized to identify conditions adverse to quality and that those
      conditions were being adequately evaluated, corrected, and trended.
  b. Findings
      No findings of significance were identified.
                                              -30-                                     Enclosure
 
4OA3 Event Followup
  1. (Closed) LER 50-458/2004-003-01, Unplanned Automatic Start of Standby Diesel
    Generator Due to Loss of Division 1 Switchgear
    On October 31, 2004, technicians caused an unexpected degraded voltage signal,
    which resulted in a loss of the Division I 4.16 kV ESF bus during preparations for the
    Division I loss of offsite power/loss of coolant accident test. The Division I EDG
    automatically started and powered the ESF bus and all equipment operated as
    expected. Initial inspection of this event was documented in NRC integrated inspection
    Report 05000458/2004005. During this inspection period, the inspectors reviewed the
    LER, the root cause analysis, and corrective actions documented in
    CR-RBS-2004-03518. No additional findings of significance were identified. This LER
    is closed.
  2. (Closed) LER 50-458/2004-004-01, Unplanned Automatic Start of Standby Diesel
    Generator Due to Loss of Division 2 Switchgear
    On November 1, 2004, technicians inadvertently caused a trip of Transformer RSS2
    preferred station service Transformer RTX-XSR1F while troubleshooting a transformer
    sudden pressure relay trip circuit. As a result, power was also lost to preferred station
    Transformer RTX-XSR1D and the Division II 4.16 kV ESF bus. The running shutdown
    cooling, alternate decay heat removal, and plant operating water cleanup systems lost
    power until the Division II EDG started and restored power to the ESF bus. Shutdown
    cooling was restored in less than one hour. Initial inspection of this event was
    documented in NRC integrated inspection Report 05000458/2004005. During this
    inspection period, the inspectors reviewed the LER, the root cause analysis, and
    corrective actions documented in CR-RBS-2004-03546. No additional findings of
    significance were identified. This LER is closed.
  3. (Closed) LER 50-458/2004-005-01, Unplanned Automatic Scram Due to Loss of
    Non-Vital 120 Volt Instrument Bus
    On December 10, 2004, an automatic scram occurred due to a loss of power to
    nonsafety-related instrumentation Bus VBN-PNL01B1. A capacitor on the control board
    for the nonsafety-related Inverter BYS-INV01B static switch failed, which caused a loss
    of power to Bus VBN-PNL01B1, a subsequent downshift of the plant operating
    recirculation pumps and a lockup of the main feedwater regulating valves. The result
    was an automatic plant scram complicated by a loss of normal feedwater. Inspection of
    this event was documented in NRC integrated inspection Report 05000458/2004005.
    Additional inspection was documented in NRC supplemental inspection Report
    05000458/2005012. During this inspection period, the inspectors reviewed the LER, the
    root cause analysis, and corrective actions documented in CR-RBS-2004-04289. No
    additional findings of significance were identified. This LER is closed.
                                              -31-                                   Enclosure
 
  4. (Closed) LER 50-458 /2005-001-01, Unplanned Manual Scram Due to Indication of
      Ground Fault in Main Generator
      On January 15, 2005, while the plant was at 100 percent power, a main generator field
      ground fault alarm was received. Control room operators tripped the turbine in
      accordance with alarm response Procedure ARP-680-09. The licensee later determined
      that one of the five rectifier banks in the generator excitation control system was the
      source of the ground and removed it from service. In addition, the licensee tested the
      relay that causes the main generator ground fault alarm and found it to be out of
      calibration such that it alarmed before the ground current reached its setpoint. The
      alarm response procedure requirement to trip the turbine was revised to allow validation
      of the alarm before tripping the main turbine. Inspection of this event was documented
      in NRC integrated inspection Report 05000458/2005002. Additional inspection was
      documented in NRC supplemental inspection Report 05000458/2005012. During this
      inspection period, the inspectors reviewed the LER, the root cause analysis, and
      corrective actions documented in CR-RBS-2005-00140. No additional findings of
      significance were identified. This LER is closed.
4OA5 Other Activities
      Implementation of Temporary Instruction 2515/165 - Operational Readiness of Offsite
      Power and Impact on Plant Risk
  a. Inspection Scope
      The objective of Temporary Instruction 2515/165, "Operational Readiness of Offsite
      Power and Impact on Plant Risk," was to gather information to support the assessment
      of nuclear power plant operational readiness of offsite power systems and impact on
      plant risk. During this inspection, the inspectors interviewed licensee personnel,
      reviewed licensee procedures, and gathered information for further evaluation by the
      Office of Nuclear Reactor Regulation.
  b. Findings
      No findings of significance were identified.
4OA6 Meetings, Including Exit
      Exit Meetings
      On May 5, 2006, the inspector presented the occupational radiation safety inspection
      results to Mr. D. Vinci, General Manager, Plant Operations, and other members of his
      staff who acknowledged the findings. The inspector confirmed that proprietary
      information was not provided or examined during the inspection.
      On May 5, 2006, the inspector presented the results of this inspection of inservice
      inspection activities to Mr. P. Russell, Manager, System Engineering, and other
                                                -32-                                   Enclosure
 
    members of licensee management. The inspector confirmed that proprietary
    information was not provided or examined during the inspection.
    On July 5, 2006, the resident inspectors presented the integrated baseline inspection
    results to Mr. P. Hinnenkamp, Vice President - Operations, and other members of
    licensee management. The inspectors confirmed that proprietary information was not
    provided or examined during the inspection.
ATTACHMENT: SUPPLEMENTAL INFORMATION
                                          -33-                                    Enclosure
 
                              SUPPLEMENTAL INFORMATION
                                  KEY POINTS OF CONTACT
Licensee Personnel
T. Baccus, Acting Supervisor, ALARA Planning
L. Ballard, Manager, Quality Programs
D. Burnett, Superintendent, Chemistry
D. Burnett, Superintendent, Chemistry
C. Bush, Manager, Outage
C. Bush, Manager, Outage
Line 623: Line 1,388:
M. Davis, Manager, Radiation Protection
M. Davis, Manager, Radiation Protection
C. Forpahl, Manager, Corrective Action Program
C. Forpahl, Manager, Corrective Action Program
T. Gates, Manager, Equipment ReliabilityH. Goodman, Director, Engineering
T. Gates, Manager, Equipment Reliability
H. Goodman, Director, Engineering
K. Higginbotham, Assistant Operations Manager - Shift
K. Higginbotham, Assistant Operations Manager - Shift
P. Hinnenkamp, Vice President - Operations
P. Hinnenkamp, Vice President - Operations
Line 635: Line 1,401:
J. Maher, Superintendent, Reactor Engineering
J. Maher, Superintendent, Reactor Engineering
W. Mashburn, Manager, Design Engineering
W. Mashburn, Manager, Design Engineering
J. Miller, Manager, Training and DevelopmentP. Russell, Manager, System Engineering
J. Miller, Manager, Training and Development
P. Russell, Manager, System Engineering
C. Stafford, Manager, Operations
C. Stafford, Manager, Operations
D. Vinci, General Manager - Plant OperationsLIST OF ITEMS OPENED, CLOSED, AND DISCUSSEDOpened and Closed05000458/2006003-01NCVFailure to identify Division III ESF bus supply breaker notracked in05000458/2006003-02NCVFailure to adequately manage an increase in plant risk 05000458/2006003-03NCVInadequate procedure to verify required offsite powerbreaker alignment05000458/2006003-04NCVFailure to control access to a high radiation area
D. Vinci, General Manager - Plant Operations
05000458/2006003-05NCV Failure to perform airborne radiation survey  
                    LIST OF ITEMS OPENED, CLOSED, AND DISCUSSED
AttachmentA-2Closed50-458/2004-003-01LERUnplanned Automatic Start of Standby Diesel GeneratorDue to Loss of Division 1 Switchgear50-458/2004-004-01LER Unplanned Automatic Start of Standby Diesel GeneratorDue to Loss of Division 2 Switchgear50-458/2004-005-01LERUnplanned Automatic Scram Due to Loss of Non-Vital 120Volt Instrument Bus50-458 /2005-001-01LERUnplanned Manual Scram Due to Indication of GroundFault in Main GeneratorLIST OF DOCUMENTS REVIEWEDThe following documents were selected and reviewed by the inspectors to accomplish theobjectives and scope of the inspection and to support any findings:Section 1R06: Inservice Inspection ActivitiesProceduresCEP-NDE-0400, "Ultrasonic Examination," Revision 0CEP-NDE-0404, "Manual Ultrasonic Examination of Ferritic Piping Welds (ASME XI),"Revision 1CEP-NDE-0407, "Straight Beam Ultrasonic Examination of Bolts and Studs (ASME XI),"Revision 1CEP-NDE-0423, "Manual Ultrasonic Examination of Austenitic Piping Welds (ASME XI),"Revision 1CEP-NDE-0424, "Manual Ultrasonic Examination of the Reactor Vessel Flange Ligament Areas(ASME XI)," Revision 1CEP-NDE-0428, "Manual Ultrasonic Throughwall Sizing in Piping Welds (ASME XI)," Revision 1
Opened and Closed
CEP-NDE-0641, "Liquid Penetrant Examination for ASME Section XI," Revision 1
05000458/2006003-01          NCV    Failure to identify Division III ESF bus supply breaker not
CEP-NDE-0731, "Magnetic Particle Examination (ASME Section XI)," Revision 0
                                    racked in
SPP-7010, "Preparation of Weld Data Documents," Revision 9  
05000458/2006003-02          NCV    Failure to adequately manage an increase in plant risk
AttachmentMiscellaneous Documents7228.000-701-131A, "Risk Informed Break Exclusion Region Evaluation for River BendStation," Revision 0Liquid Penetrant ExaminationsBOP-PT-06-024BOP-PT-06-025BOP-PT-06-026BOP-PT-06-029UT Calibration ReportsCAL -06-015CAL -06-016CAL-06-017UT Pipe Weld ExaminationsISI-UT-06-003ISI-UT-06-006ISI-UT-06-009ISI-UT-06-012ISI-UT-06-004ISI-UT-06-007ISI-UT-06-010ISI-UT-06-013
05000458/2006003-03          NCV    Inadequate procedure to verify required offsite power
ISI-UT-06-005ISI-UT-06-008ISI-UT-06-011ISI-UT-06-014Condition ReportsCR-RBS-2005-00065CR-RBS-2005-00067CR-RBS-2005-00100CR-RBS-2005-01379Section 1R15: Operability EvaluationsPrimary Containment Purge Exhaust Line OperabilityCR-RBS-2006-00964, primary containment purge exhaust line leak rate test results showingnegative trendADM-0050, "Primary Containment Leakage Rate Testing Program," Revision 8
                                    breaker alignment
SEP-APJ-001, "Primary containment Leakage Rate Testing (Appendix J) Program,"Revision 0GSTP-403-7301, "Containment Purge System Isolation Valve Leak Rate Test," Revisions 0, 1, 2, and 3RBS-ER-00-0589, "Post RF-09 LLRT Testing Interval Determination," dated January 25, 2001
05000458/2006003-04          NCV    Failure to control access to a high radiation area
05000458/2006003-05          NCV    Failure to perform airborne radiation survey
                                              A-1                                    Attachment
 
Closed
50-458/2004-003-01          LER    Unplanned Automatic Start of Standby Diesel Generator
                                    Due to Loss of Division 1 Switchgear
50-458/2004-004-01          LER    Unplanned Automatic Start of Standby Diesel Generator
                                    Due to Loss of Division 2 Switchgear
50-458/2004-005-01          LER    Unplanned Automatic Scram Due to Loss of Non-Vital 120
                                    Volt Instrument Bus
50-458 /2005-001-01          LER    Unplanned Manual Scram Due to Indication of Ground
                                    Fault in Main Generator
                              LIST OF DOCUMENTS REVIEWED
The following documents were selected and reviewed by the inspectors to accomplish the
objectives and scope of the inspection and to support any findings:
Section 1R06: Inservice Inspection Activities
Procedures
CEP-NDE-0400, Ultrasonic Examination, Revision 0
CEP-NDE-0404, Manual Ultrasonic Examination of Ferritic Piping Welds (ASME XI),
Revision 1
CEP-NDE-0407, Straight Beam Ultrasonic Examination of Bolts and Studs (ASME XI),
Revision 1
CEP-NDE-0423, Manual Ultrasonic Examination of Austenitic Piping Welds (ASME XI),
Revision 1
CEP-NDE-0424, Manual Ultrasonic Examination of the Reactor Vessel Flange Ligament Areas
(ASME XI), Revision 1
CEP-NDE-0428, Manual Ultrasonic Throughwall Sizing in Piping Welds (ASME XI), Revision 1
CEP-NDE-0641, Liquid Penetrant Examination for ASME Section XI, Revision 1
CEP-NDE-0731, Magnetic Particle Examination (ASME Section XI), Revision 0
SPP-7010, Preparation of Weld Data Documents, Revision 9
                                              A-2                                Attachment
 
Miscellaneous Documents
7228.000-701-131A, Risk Informed Break Exclusion Region Evaluation for River Bend
Station, Revision 0
Liquid Penetrant Examinations
BOP-PT-06-024        BOP-PT-06-025        BOP-PT-06-026          BOP-PT-06-029
UT Calibration Reports
CAL -06-015                  CAL -06-016                  CAL-06-017
UT Pipe Weld Examinations
ISI-UT-06-003        ISI-UT-06-006        ISI-UT-06-009          ISI-UT-06-012
ISI-UT-06-004        ISI-UT-06-007        ISI-UT-06-010          ISI-UT-06-013
ISI-UT-06-005        ISI-UT-06-008        ISI-UT-06-011          ISI-UT-06-014
Condition Reports
CR-RBS-2005-00065    CR-RBS-2005-00067    CR-RBS-2005-00100      CR-RBS-2005-01379
Section 1R15: Operability Evaluations
Primary Containment Purge Exhaust Line Operability
CR-RBS-2006-00964, primary containment purge exhaust line leak rate test results showing
negative trend
ADM-0050, Primary Containment Leakage Rate Testing Program, Revision 8
SEP-APJ-001, Primary containment Leakage Rate Testing (Appendix J) Program,
Revision 0G
STP-403-7301, Containment Purge System Isolation Valve Leak Rate Test, Revisions 0, 1, 2,
and 3
RBS-ER-00-0589, Post RF-09 LLRT Testing Interval Determination, dated January 25, 2001
RBS TS Amendment 81, dated July 20, 1995
RBS TS Amendment 81, dated July 20, 1995
RBS TS Bases Revision 126, dated March 31, 206  
RBS TS Bases Revision 126, dated March 31, 206
AttachmentA-4NNS-ACB23 Not FunctionalElectrical DrawingsEE-001AC, "Startup Electrical Distribution Chart," Revision 33ESK-05NNS03, "Elementary Diagram - 4.16 kV Switchgear Bus 1C Normal Supply ACB,"Revision 13Corrective Action DocumentsCR-RBS-2006-02402CR-RBS-2006-0235CR-RBS-2006-02337CR-RBS-1998-00190ProceduresOSP-0022, "Operations General Administrative Guidelines," Revision 01GOP-0001, "Plant Startup," Revision 47, performed on May 12, 2006STP-000-0102, "Power Distribution Alignment Check," Revision 4, performed on May 9, 2006
                                                                                Attachment
STP-000-0102, "Power Distribution Alignment Check," Revision 4, performed on May 22, 2006Work RequestsWR 76625WR 77441WR77478
 
Miscellaneous DocumentsMain Control Room LogsTS LCO Records: 1-OPT-06-01871-TS-06-0694
NNS-ACB23 Not Functional
RBS Tagout Record: 1-302-NNS-SWG1A-006-ASection 1R20: Refueling and Other Outage ActivitiesProceduresRSP-0217, "Auxiliary Access Control Functions," Revision 27GOP-0003, "Scram Recovery," Revision 14A, post scram report, dated April 23, 2006
Electrical Drawings
OSP-0031, "Shutdown Operations Protection Plan," Revision 16OSP-0041, "Alternate Decay Heat Removal," Revision 8A
EE-001AC, Startup Electrical Distribution Chart, Revision 33
AOP-0051, "Loss of Decay Heat Removal," Revision 18
ESK-05NNS03, Elementary Diagram - 4.16 kV Switchgear Bus 1C Normal Supply ACB,
OSP-0034, "Control of Obstructions for Primary Containment/Fuel Building Operability,"Revision 3  
Revision 13
AttachmentA-5GOP-0001, "Plant Startup," Revision 47, performed on May 12, 2006Corrective Action DocumentsCR-RBS-2006-00691CR-RBS-2006-01937
Corrective Action Documents
Miscellaneous DocumentsControl Room Logs
CR-RBS-2006-02402          CR-RBS-2006-0235              CR-RBS-2006-02337
CR-RBS-1998-00190
Procedures
OSP-0022, Operations General Administrative Guidelines, Revision 01
GOP-0001, Plant Startup, Revision 47, performed on May 12, 2006
STP-000-0102, Power Distribution Alignment Check, Revision 4, performed on May 9, 2006
STP-000-0102, Power Distribution Alignment Check, Revision 4, performed on May 22, 2006
Work Requests
WR 76625            WR 77441              WR77478
Miscellaneous Documents
Main Control Room Logs
TS LCO Records: 1-OPT-06-0187 1-TS-06-0694
RBS Tagout Record: 1-302-NNS-SWG1A-006-A
Section 1R20: Refueling and Other Outage Activities
Procedures
RSP-0217, Auxiliary Access Control Functions, Revision 27
GOP-0003, Scram Recovery, Revision 14A, post scram report, dated April 23, 2006
OSP-0031, Shutdown Operations Protection Plan, Revision 16
OSP-0041, Alternate Decay Heat Removal, Revision 8A
AOP-0051, Loss of Decay Heat Removal, Revision 18
OSP-0034, Control of Obstructions for Primary Containment/Fuel Building Operability,
Revision 3
                                              A-4                                Attachment
 
GOP-0001, Plant Startup, Revision 47, performed on May 12, 2006
Corrective Action Documents
CR-RBS-2006-00691          CR-RBS-2006-01937
Miscellaneous Documents
Control Room Logs
TS LCO Logs
TS LCO Logs
Daily Refueling Outage Updates
Daily Refueling Outage Updates
ORAT Report
ORAT Report
WO 50340401 and 81284
WO 50340401 and 81284
ER-RB-2005-0157-000, "Install new relays on the output of EOC-RPT optical output cardsC71A-AT17 and C71A-AT18," dated May 16, 2006WO 5034041's task outline to configure the station blackout diesel to supply power to spent fuelpool cooling Pump SFC-P1AWO 5034041, Configure the station blackout diesel to supply power to spent fuel pool coolingPump SFC-P1A, written May 3, 2006Section 1R22: Surveillance TestingDrawing EE-001AC, "Startup Electrical Distribution Chart," Revision 33TS Section 3.8.1 and Bases 3.8.1, Revision 0
ER-RB-2005-0157-000, Install new relays on the output of EOC-RPT optical output cards
USAR Section 8.2.1.2.1, "General Design Criteria," Revision 16
C71A-AT17 and C71A-AT18, dated May 16, 2006
NUREG-0989, "Safety Evaluation Report Related to the Operation of River Bend Station,"dated May 1984TS LCO Logs1-TS-06-0694I-TS-06-06851-TS-05-0386
WO 5034041's task outline to configure the station blackout diesel to supply power to spent fuel
Corrective Action DocumentsCR-RBS-2006-02675CR-RBS-2006-02402CR-RBS-2005-02331  
pool cooling Pump SFC-P1A
AttachmentA-6Section 4OA2: Identification and Resolution of ProblemsSemiannual Trend ReviewCR-RBS-2004-02165CR-RBS-2006-00159
WO 5034041, Configure the station blackout diesel to supply power to spent fuel pool cooling
CR-RBS-2006-00226
Pump SFC-P1A, written May 3, 2006
CR-RBS-2006-00279
Section 1R22: Surveillance Testing
CR-RBS-2006-00296
Drawing EE-001AC, Startup Electrical Distribution Chart, Revision 33
CR-RBS-2006-00434
TS Section 3.8.1 and Bases 3.8.1, Revision 0
CR-RBS-2006-00663
USAR Section 8.2.1.2.1, General Design Criteria, Revision 16
CR-RBS-2006-00798
NUREG-0989, Safety Evaluation Report Related to the Operation of River Bend Station,
CR-RBS-2006-00799
dated May 1984
CR-RBS-2006-00928
TS LCO Logs
CR-RBS-2006-00993
1-TS-06-0694        I-TS-06-0685          1-TS-05-0386
CR-RBS-2006-01131
Corrective Action Documents
CR-RBS-2006-01132
CR-RBS-2006-02675          CR-RBS-2006-02402              CR-RBS-2005-02331
CR-RBS-2006-01205
                                            A-5                                  Attachment
CR-RBS-2006-01261CR-RBS-2006-01270CR-RBS-2006-01324
 
CR-RBS-2006-01333
Section 4OA2: Identification and Resolution of Problems
CR-RBS-2006-01429
Semiannual Trend Review
CR-RBS-2006-01464
CR-RBS-2004-02165                CR-RBS-2006-01270              CR-RBS-2006-02469
CR-RBS-2006-01489
CR-RBS-2006-00159                CR-RBS-2006-01324              CR-RBS-2006-02484
CR-RBS-2006-01490
CR-RBS-2006-00226                CR-RBS-2006-01333              CR-RBS-2006-02540
CR-RBS-2006-02269
CR-RBS-2006-00279                CR-RBS-2006-01429              CR-RBS-2006-02544
CR-RBS-2006-02348
CR-RBS-2006-00296                CR-RBS-2006-01464              CR-RBS-2006-02550
CR-RBS-2006-02349
CR-RBS-2006-00434                CR-RBS-2006-01489              CR-RBS-2006-02558
CR-RBS-2006-02356
CR-RBS-2006-00663                CR-RBS-2006-01490              CR-RBS-2006-02559
CR-RBS-2006-02375
CR-RBS-2006-00798                CR-RBS-2006-02269               CR-RBS-2006-02651
CR-RBS-2006-02406
CR-RBS-2006-00799                CR-RBS-2006-02348              CR-RBS-2006-02661
CR-RBS-2006-02407CR-RBS-2006-02469CR-RBS-2006-02484
CR-RBS-2006-00928                CR-RBS-2006-02349              CR-RBS-2006-02682
CR-RBS-2006-02540
CR-RBS-2006-00993                CR-RBS-2006-02356              CR-RBS-2006-02683
CR-RBS-2006-02544
CR-RBS-2006-01131                CR-RBS-2006-02375              CR-RBS-2006-02732
CR-RBS-2006-02550
CR-RBS-2006-01132                CR-RBS-2006-02406              CR-RBS-2006-02733
CR-RBS-2006-02558
CR-RBS-2006-01205                CR-RBS-2006-02407              CR-RBS-2006-02799
CR-RBS-2006-02559
CR-RBS-2006-01261
CR-RBS-2006-02651
Section 2OS1: Access Controls to Radiologically Significant Areas
CR-RBS-2006-02661
Corrective Action Documents
CR-RBS-2006-02682
CR-RBS-2006-00090 CR-RBS- 2006-01294 CR-RBS-2006-01787 CR-RBS- 2006-01950
CR-RBS-2006-02683
Radiation Work Permits
CR-RBS-2006-02732
2006-1915      RFO-13, Remove and Replace LPRMs, Including Support Activities
CR-RBS-2006-02733
2006-1921      RFO-13, Flow Control Valve Maintenance, Including Support Activities
CR-RBS-2006-02799Section 2OS1: Access Controls to Radiologically Significant Areas
2006-1929      RFO-13, Recirc Pump Work, Including Support Activities
Corrective Action DocumentsCR-RBS-2006-00090   CR-RBS- 2006-01294   CR-RBS-2006-01787   CR-RBS- 2006-01950Radiation Work Permits2006-1915RFO-13, Remove and Replace LPRMs, Including Support Activities2006-1921RFO-13, Flow Control Valve Maintenance, Including Support Activities
Procedures
2006-1929RFO-13, Recirc Pump Work, Including Support ActivitiesProceduresRP-103Access Control, Revision 2RP-106Radiological Survey Documentation, Revision 1
RP-103        Access Control, Revision 2
RP-108Radiation Protection Posting, Revision 2
RP-106        Radiological Survey Documentation, Revision 1
RPP-0006Performance of Radiological Surveys, Revision 19Section 2OS2: ALARA Planning and Controls (71121.02)Corrective Action DocumentsCR-RBS-2006-01746ProceduresENS-RP-105Radiation Work Permits, Revision 7  
RP-108        Radiation Protection Posting, Revision 2
AttachmentA-7LIST OF ACRONYMSCDFcore damage frequencyALARAas low as is reasonably achievable
RPP-0006      Performance of Radiological Surveys, Revision 19
ASMEAmerican Society of Mechanical Engineers
Section 2OS2: ALARA Planning and Controls (71121.02)
CAPcorrective action program
Corrective Action Documents
CR-RBS-2006-01746
Procedures
ENS-RP-105 Radiation Work Permits, Revision 7
                                              A-6                                Attachment


CFRCode of Federal RegulationsCR-RBSRiver Bend Station condition report
                              LIST OF ACRONYMS
EDGemergency diesel generator
CDF    core damage frequency
LERlicensee event report
ALARA  as low as is reasonably achievable
MCinspection manual chapter
ASME  American Society of Mechanical Engineers
NCVnoncited violation
CAP    corrective action program
NDEnondestructive examination
CFR    Code of Federal Regulations
NEINuclear Energy Institute
CR-RBS River Bend Station condition report
NRCU.S. Nuclear Regulatory Commission
EDG    emergency diesel generator
ORAToutage risk assessment team
LER    licensee event report
PIperformance indicators
MC    inspection manual chapter
RCSreactor coolant system
NCV    noncited violation
RFOrefueling outage
NDE    nondestructive examination
SFCspent fuel pool cooli ng syst emSOPsystem operating proceduresSRsurveillance requirement
NEI    Nuclear Energy Institute
SSCstructures, systems, or componentsSTPsurveillance test procedure
NRC    U.S. Nuclear Regulatory Commission
TSTechnical Specifications
ORAT  outage risk assessment team
USARUpdated Safety Analysis Report
PI    performance indicators
WOwork order
RCS    reactor coolant system
WRwork request
RFO    refueling outage
SFC    spent fuel pool cooling system
SOP    system operating procedures
SR    surveillance requirement
SSC    structures, systems, or components
STP    surveillance test procedure
TS    Technical Specifications
USAR  Updated Safety Analysis Report
WO    work order
WR    work request
                                      A-7      Attachment
}}
}}

Revision as of 15:02, 23 November 2019

IR 05000458/2006003; 04/01/2006 - 06/30/2006; River Bend Station; Operability Evaluations, Refueling and Other Outage Activities, Surveillance Testing, Occupational Radiation Safety
ML062260238
Person / Time
Site: River Bend Entergy icon.png
Issue date: 08/14/2006
From: Kennedy K
NRC/RGN-IV/DRP/RPB-C
To: Hinnenkamp P
Entergy Operations
References
IR-06-003
Download: ML062260238 (45)


See also: IR 05000458/2006003

Text

August 14, 2006

Paul D. Hinnenkamp

Vice President - Operations

Entergy Operations, Inc.

River Bend Station

5485 US Highway 61N

St. Francisville, LA 70775

SUBJECT: RIVER BEND STATION - NRC INTEGRATED INSPECTION

REPORT 05000458/2006003

Dear Mr. Hinnenkamp:

On June 30, 2006, the U.S. Nuclear Regulatory Commission (NRC) completed an inspection at

your River Bend Station. The enclosed integrated inspection report documents the inspection

results, which were discussed on July 5, 2006, with you and other members of your staff.

The inspection examined activities conducted under your license as they relate to safety and

compliance with the Commissions rules and regulations and with the conditions of your license.

The inspectors reviewed selected procedures and records, observed activities, and interviewed

personnel.

The report documents three NRC-identified findings and two self-revealing findings of very low

safety significance (Green). The NRC has also determined that violations are associated with

these findings. However, because these violations were of very low safety significance and

were entered into your corrective action program, the NRC is treating these violations as

noncited violations, consistent with Section VI.A.1 of the NRC Enforcement Policy. If you

contest the violations or the significance of the violations, you should provide a response within

30 days of the date of this inspection report, with the basis for your denial, to the U.S. Nuclear

Regulatory Commission, ATTN: document Control Desk, Washington, DC 20555-0001, with

copies to the Regional Administrator, U.S. Nuclear Regulatory Commission, Region IV, 611

Ryan Plaza Drive, Suite 400, Arlington, Texas 76011-4005; the Director, Office of Enforcement,

U.S. Nuclear Regulatory Commission, Washington, DC 20555-0001; and the NRC Resident

Inspector at the River Bend Station facility.

In accordance with 10 CFR 2.390 of the NRCs Rules of Practice, a copy of this letter, its

enclosure, and your response (if any) will be available electronically for public inspection in the

NRC Public Document Room or from the Publicly Available Records (PARS) component of

NRCs document system (ADAMS). ADAMS is accessible from the NRC Website at

http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room).

Entergy Operations, Inc. -2-

Should you have any questions concerning this inspection, we will be pleased to discuss them

with you.

Sincerely,

/RA/

Kriss M. Kennedy, Chief

Project Branch C

Division of Reactor Projects

Docket: 50-458

License: NPF-47

Enclosure:

NRC Inspection Report 05000458/2006003

w/Attachment: Supplemental Information

cc w/enclosure:

Senior Vice President and

Chief Operating Officer

Entergy Operations, Inc.

P.O. Box 31995

Jackson, MS 39286-1995

Vice President

Operations Support

Entergy Operations, Inc.

P.O. Box 31995

Jackson, MS 39286-1995

General Manager

Plant Operations

Entergy Operations, Inc.

River Bend Station

5485 US Highway 61N

St. Francisville, LA 70775

Director - Nuclear Safety

Entergy Operations, Inc.

River Bend Station

5485 US Highway 61N

St. Francisville, LA 70775

Wise, Carter, Child & Caraway

P.O. Box 651

Jackson, MS 39205

Entergy Operations, Inc. -3-

Winston & Strawn LLP

1700 K Street, N.W.

Washington, DC 20006-3817

Manager - Licensing

Entergy Operations, Inc.

River Bend Station

5485 US Highway 61N

St. Francisville, LA 70775

The Honorable Charles C. Foti, Jr.

Attorney General

Department of Justice

State of Louisiana

P.O. Box 94005

Baton Rouge, LA 70804-9005

H. Anne Plettinger

3456 Villa Rose Drive

Baton Rouge, LA 70806

Bert Babers, President

West Feliciana Parish Police Jury

P.O. Box 1921

St. Francisville, LA 70775

Richard Penrod, Senior Environmental

Scientist

Office of Environmental Services

Northwestern State University

Russell Hall, Room 201

Natchitoches, LA 71497

Brian Almon

Public Utility Commission

William B. Travis Building

P.O. Box 13326

1701 North Congress Avenue

Austin, TX 78711-3326

Entergy Operations, Inc. -4-

Chairperson

Denton Field Office

Chemical and Nuclear Preparedness

and Protection Division

Office of Infrastructure Protection

Preparedness Directorate

Dept. of Homeland Security

800 North Loop 288

Federal Regional Center

Denton, TX 76201-3698

Entergy Operations, Inc. -5-

Electronic distribution by RIV:

Regional Administrator (BSM1)

DRP Director (ATH)

DRS Director (DDC)

DRS Deputy Director (RJC1)

Senior Resident Inspector (PJA)

Branch Chief, DRP/C (KMK)

Senior Project Engineer, DRP/C (WCW)

Team Leader, DRP/TSS (RLN1)

RITS Coordinator (KEG)

DRS STA (DAP)

J. Lamb, OEDO RIV Coordinator (JGL1)

ROPreports

RBS Site Secretary (LGD)

W. A. Maier, RSLO (WAM)

SUNSI Review Completed: __wcw_ ADAMS: : Yes G No Initials: __wcw___

Publicly Available G Non-Publicly Available G Sensitive  : Non-Sensitive

R:\_REACTORS\_RB\2006\RB2006-03RP-PJA.wpd

RIV:SRI:DRP/C RI:DRP/C C:DRS/OB C:DRS/EB1 C:DRS/PSB

PJAlter MOMiller ATGody JAClark MPShannon

T - WCWalker E - WCWalker /RA/ /RA/ /RA/

8/10/06 8/10/06 8/11/06 8/10/06 8/10/06

C:DRS/EB2 SRA:DRS C:DRP/C

LJSmith DPLoveless KMKennedy

/RA/ /RA/ /RA/

8/10/06 8/14/06 8/14/06

OFFICIAL RECORD COPY T=Telephone E=E-mail F=Fax

U.S. NUCLEAR REGULATORY COMMISSION

REGION IV

Docket: 50-458

License: NPF-47

Report: 05000458/2006003

Licensee: Entergy Operations, Inc.

Facility: River Bend Station

Location: 5485 U.S. Highway 61

St. Francisville, Louisiana

Dates: April 1 to June 30, 2006

Inspectors: P. Alter, Senior Resident Inspector, Project Branch C

M. Miller, Resident Inspector, Project Branch C

G. Werner, Senior Project Engineer, Project Branch D

L. Ricketson, P.E., Senior Health Physicist, Plant Support Branch

W. Sifre, Senior Reactor Inspector, Engineering Branch 1

Approved By: Kriss M. Kennedy, Chief

Project Branch C

Division of Reactor Projects

-1- Enclosure

TABLE OF CONTENTS

SUMMARY OF FINDINGS . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 3

REPORT DETAILS . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 6

REACTOR SAFETY . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 6

1R01 Adverse Weather Protection . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 6

1R04 Equipment Alignment . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 7

1R05 Fire Protection . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 7

1R08 Inservice Inspection Activities . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 8

1R11 Licensed Operator Requalification Program . . . . . . . . . . . . . . . . . . . . . . . . . . . 9

1R12 Maintenance Effectiveness . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 10

1R13 Maintenance Risk Assessments and Emergent Work Control . . . . . . . . . . . . . 10

1R14 Operator Performance During Nonroutine Evolutions and Events . . . . . . . . . . 11

1R15 Operability Evaluations . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 12

1R19 Postmaintenance Testing . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 17

1R20 Refueling and Other Outage Activities . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 17

1R22 Surveillance Testing . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 20

1R23 Temporary Plant Modifications . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 23

1EP6 Drill Evaluation . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 23

RADIATION SAFETY . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 24

2OS1 Access Control to Radiologically Significant Areas . . . . . . . . . . . . . . . . . . . . . 24

2OS2 ALARA Planning and Controls . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 27

OTHER ACTIVITIES . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 28

4OA1 Performance Indicator (PI) Verification . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 28

4OA2 Identification and Resolution of Problems . . . . . . . . . . . . . . . . . . . . . . . . . . . . 29

4OA3 Event Followup . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 31

4OA5 Other Activities . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 32

4OA6 Meetings, Including Exit . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 32

SUPPLEMENTAL INFORMATION . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . A-1

KEY POINTS OF CONTACT . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . A-1

LIST OF ITEMS OPENED, CLOSED, AND DISCUSSED . . . . . . . . . . . . . . . . . . . . . . . . . . . A-1

LIST OF DOCUMENTS REVIEWED . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . A-2

LIST OF ACRONYMS . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . A-7

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SUMMARY OF FINDINGS

IR 05000458/2006003; 04/01/2006 - 06/30/2006; River Bend Station; Operability Evaluations,

Refueling and Other Outage Activities, Surveillance Testing, Occupational Radiation Safety.

The report covered a 3-month period of routine baseline inspections by resident inspectors and

announced baseline inspections by regional engineering and radiation protection inspectors.

Five Green noncited violations were identified. The significance of most findings is indicated by

their color (Green, White, Yellow, Red) using Inspection Manual Chapter 0609, Significance

Determination Process. Findings for which the significance determination process does not

apply may be Green or be assigned a severity level after NRC management review. The

NRCs program for overseeing the safe operation of commercial nuclear power reactors is

described in NUREG-1649, Reactor Oversight Process, Revision 3, dated July 2000.

A. NRC-Identified and Self-Revealing Findings

Cornerstone: Mitigating Systems

Green. A self-revealing noncited violation of 10 CFR Part 50, Appendix B, Criterion XVI,

"Corrective Action," was reviewed involving the failure of the licensee to identify that the

normal supply breaker to the Division III 4.16 kV engineered safety features bus was not

properly racked in for a period of 24 days following maintenance. This issue was

entered into the licensee's corrective action program as CR-RBS-2006-02402.

The finding was more than minor because it was associated with the mitigating system

cornerstone attribute of configuration control and affected the associated cornerstone

objective to ensure the availability, reliability, and capability of systems that respond to

initiating events to prevent undesirable consequences. Utilizing Manual Chapter 0609,

"Significance Determination Process," a Phase 3 analysis concluded that the finding

was of very low safety significance. The cause of the finding was related to the

crosscutting aspect of problem identification and resolution in that the licensee failed to

properly evaluate available indications to identify that the breaker was not properly

racked in. (Section 1R15).

Green. An NRC identified noncited violation of 10 CFR 50.65 Maintenance Rule

Section (a)(4) was identified for the failure of the licensee to provide prescribed

compensatory measures for two Orange shutdown risk conditions during Refueling

Outage 13. Specifically, the preoutage risk assessment recommended that two work

orders be in place for maintenance electricians to provide power to one spent fuel pool

cooling pump in the event of problems with the running pump during periods of electrical

bus maintenance. The inspectors found that the work packages were not in place

before entering shutdown risk condition Orange on April 26, 2006, during the Division II

engineering safety features bus testing, and May 3, 2006, during the Division I

engineered safety features bus outage. This issue was entered into the licensee's

corrective action program as CR-RBS-2006-01937.

The finding was more than minor because the licensee failed to implement a prescribed

compensatory measure during the highest risk condition of Refueling Outage 13. The

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specific compensatory measures were called for in the preoutage risk assessment and

the shutdown operations protection plan. The finding affected the mitigating system

cornerstone because of the increased risk of a sustained loss of spent fuel pool cooling

during core offloading operations. The finding could not be evaluated using the

significance determination process, therefore the finding was reviewed by regional

management and determined to be of very low safety significance. Factors that were

considered included: (1) electrical maintenance technicians had previously performed

the task of providing alternate power to a spent fuel pool cooling pump, (2) the

necessary equipment was staged as part of the abnormal operating procedure for loss

of decay heat removal, and (3) the relatively long time to boil of the spent fuel storage

pool at that time during the refueling outage. The cause of the finding was related to the

crosscutting aspect of human performance because the licensees planned

maintenance activities and the predetermined increase in outage risk was not effectively

managed by prescribed compensatory measures (Section 1R20).

Green. An NRC identified noncited violation of Technical Specification 5.4.1.a was

identified for the failure of the licensee to provide an adequate surveillance test

procedure to perform Technical Specification Surveillance Requirement 3.8.1.1.

Specifically, STP-000-0102, Power Distribution Alignment Check, Revision 4, did not

verify the required offsite power circuit breaker alignment and indicated power

availability for the Division III 4.16 kV engineered safety features bus as required in

Modes 1, 2, and 3. This issue was entered into the licensee's corrective action program

as CR-RBS-2006-02675 and -02402.

The finding was more than minor because it was associated with the mitigating system

cornerstone attribute of configuration control and affected the associated cornerstone

objective to ensure the availability, reliability, and capability of systems that respond to

initiating events to prevent undesirable consequences. Utilizing Manual Chapter 0609,

"Significance Determination Process," a Phase 3 analysis concluded that the finding

was of very low safety significance. (Section 1R22).

Cornerstone: Occupational Radiation Safety

  • Green. The inspector reviewed a self-revealing noncited violation of Technical

Specification 5.7.1, resulting from the licensees failure to control access to a high

radiation area. While transferring reverse osmosis system filters in the radwaste

building, the licensee allowed two workers to inadvertently enter a high radiation area.

This occurred after a guard prematurely left his post in front of the 123 foot elevation

elevator door. The highest dose rate recorded by an electronic alarming dosimeter was

164 millirem per hour. The guard returned and evacuated the workers before they

accrued additional radiation dose. Planned corrective action was still being evaluated by

the licensee at the conclusion of the inspection.

The finding was more than minor because it was associated with the occupational

radiation safety attribute of exposure control and affected the cornerstone objective in

that not controlling a high radiation area could increase personal exposure. Using the

Occupational Radiation Safety Significance Determination Process, the inspector

determined that the finding was of very low safety significance because it did not

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involve: (1) an as low as is reasonably achievable finding, (2) an overexposure, (3) a

substantial potential for overexposure, or (4) an impaired ability to assess dose.

Additionally, this finding had crosscutting aspects associated with human performance

in that the failure of the individual to guard the elevator door directly contributed to the

violation. (Section 2OS1)

  • Green. The inspector identified a noncited violation of 10 CFR 20.1501(a) because the

license failed to survey airborne radioactivity. During the removal of local power range

monitors, the licensee started collecting an air sample of the work area, but discarded

the sample before analyzing it. Successful passage through the portal monitors at the

exit of the controlled access area confirmed that no worker experienced an uptake of

radioactive material. Planned corrective action is still being evaluated.

The finding was more than minor because it was associated with the occupational

radiation safety program attribute of exposure control and affected the cornerstone

objective in that the lack of knowledge of radiological conditions could increase

personnel dose. Using the Occupational Radiation Safety Significance Determination

Process, the inspector determined that the finding was of very low safety significance

because it did not involve: (1) an as low as is reasonably achievable finding, (2) an

overexposure, (3) a substantial potential for overexposure, or (4) an impaired ability to

assess dose. Additionally, this finding had crosscutting aspects associated with human

performance in that the failure to maintain the sample for analysis directly contributed to

the violation. (Section 2OS1)

B. Licensee-Identified Violations

None.

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REPORT DETAILS

Summary of Plant Status: The reactor was operated at 100 percent power from April 1-15,

2006, when the reactor scrammed due to a control circuit failure which caused both reactor

recirculation pumps to shift to slow speed. The reactor was restarted on April 17 and attained

100 percent power on April 18. On April 23, the reactor was shut down for Refueling Outage

(RFO) -13. On May 12, the reactor was restarted and attained 100 percent power on May 18.

On June 15, reactor power was reduced to 23 percent because of a problem with the main

turbine bypass valves. The reactor was returned to 100 percent power on June 18. The

reactor remained at 100 percent power for the remainder of the inspection period, with the

exception of regularly scheduled power reductions for control rod pattern adjustments and

turbine testing.

1. REACTOR SAFETY

Cornerstones: Initiating Events, Mitigating Systems, Barrier Integrity, Emergency

Preparedness

1R01 Adverse Weather Protection

a. Inspection Scope

Hurricane Season Preparations

During the week of June 12, 2006, the inspectors completed a review of the licensee's

readiness for seasonal susceptibilities involving high winds at the beginning of hurricane

season. The inspectors reviewed Procedure ENS-EP-302, Severe Weather

Response, Revision 4. The inspectors: (1) reviewed plant procedures, the Updated

Safety Analysis Report (USAR), and Technical Specifications (TS) to verify that operator

actions defined in adverse weather procedures maintained the readiness of essential

systems; (2) walked down portions of the protected area to verify that hurricane season

preparations were sufficient to support operability of essential systems, including the

ability to perform safe shutdown functions; (3) evaluated operator staffing levels to verify

the licensee could maintain the readiness of essential systems required by plant

procedures; and (4) reviewed the corrective action program (CAP) to determine if the

licensee identified and corrected problems related to adverse weather conditions.

The inspectors completed one inspection sample.

b. Findings

No findings of significance were identified.

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1R04 Equipment Alignment

Partial System Walkdowns

a. Inspection Scope

The inspectors: (1) walked down portions of the three risk important systems listed

below and reviewed system operating procedures (SOPs), piping and instrument

diagrams, and other documents to verify that critical portions of the selected systems

were correctly aligned; and (2) compared deficiencies identified during the walkdown to

the licensee's USAR and CAP to verify problems were being identified and corrected.

shutdown cooling system during refueling operations, on May 2, 2006

was out of service for maintenance, on June 12, 2006

service for planned maintenance, on June 21, 2006

Documents reviewed by the inspectors included:

Revision 16

  • SOP-0053, Standby Diesel Generator and Auxiliaries, Revision 44A

The inspectors completed three inspection samples.

h. Findings

No findings of significance were identified.

1R05 Fire Protection

b. Inspection Scope

The inspectors walked down the six plant areas listed below to assess the material

condition of active and passive fire protection features and their operational lineup and

readiness. The inspectors: (1) verified that transient combustibles were controlled in

accordance with plant procedures; (2) observed the condition of fire detection devices to

verify they remained functional; (3) observed fire suppression systems to verify they

remained functional and that access to manual actuators was unobstructed; (4) verified

that fire extinguishers and hose stations were provided at their designated locations and

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that they were in a satisfactory condition; (5) verified that passive fire protection features

(electrical raceway barriers, fire doors, fire dampers, steel fire proofing, penetration

seals, and oil collection systems) were in a satisfactory material condition; (6) verified

that adequate compensatory measures were established for degraded or inoperable fire

protection features and that the compensatory measures were commensurate with the

significance of the deficiency; and (7) reviewed the CAP to determine if the licensee

identified and corrected fire protection problems.

  • Auxiliary building piping Tunnel D, Fire Area AB-7, on May 9, 2006
  • Low pressure core spray pump room, Fire Area AB-6/Z-1, on May 9, 2006
  • Control building standby switchgear Room 1A, Fire Area C-15, on June 22, 2006
  • Control building safety related cable tray area and stairway Number 3, Fire Area

C-16 and C-29, on June 22, 2006

  • Division I EDG control and diesel engine rooms, Fire Area DG-6/Z-1, on June 22,

2006

Documents reviewed by the inspectors included:

  • Pre-Fire Plan/Strategy Book
  • USAR Section 9A.2, Fire Hazards Analysis, Revision 10

The inspectors completed six inspection samples.

b. Findings

No findings of significance were identified.

1R08 Inservice Inspection Activities

a. Inspection Scope

The inspector witnessed the performance of 12 volumetric (ultrasonic) and four surface

(liquid penetrant) examinations. The sample of nondestructive examination (NDE)

activities is listed in the attachment.

For each of the NDE activities reviewed, the inspector verified that the examinations

were performed in accordance with American Society of Mechanical Engineers (ASME)

Code requirements.

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During the review of each examination, the inspector verified that appropriate NDE

procedures were used, that examinations and conditions were as specified in the

procedure, and that test instrumentation or equipment was properly calibrated and within

the allowable calibration period. The inspector also reviewed documentation to verify

that indications revealed by the examinations were dispositioned in accordance with the

ASME Code specified acceptance standards.

The inspector verified the certifications of the NDE personnel observed performing

examinations or identified during review of completed examination packages.

The inspection procedure requires review of one or two examinations from the previous

outage with recordable indications that were accepted for continued service to ensure

that the disposition was done in accordance with the ASME Code. There were no

recordable indications that required evaluation during the last outage.

If the licensee completed welding on the pressure boundary for Class 1 or 2 systems

since the beginning of the previous outage, the procedure requires verification that

acceptance and preservice examinations were done in accordance with the ASME Code

for one to three welds. There were no welds available for review.

The procedure also requires verification that one or two ASME Code Section XI repairs

or replacements meet code requirements. There were no code repairs or replacements

available at the time of this inspection.

The inspectors completed 16 inspection samples.

b. Findings

No findings of significance were identified.

1R11 Licensed Operator Requalification Program

a. Inspection Scope

On June 13, 2006, the inspectors observed testing and training of senior reactor

operators and reactor operators to verify the adequacy of training, to assess operator

performance, and to assess the evaluators critique. The training evaluation scenario

observed was RSMS-OPS-422, Loss of Circ Water Pump, Failure of Steam Flow

Transmitter and Instrument Air System Leak, Revision 4.

The inspectors completed one inspection sample.

b. Findings

No findings of significance were identified.

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1R12 Maintenance Effectiveness

a. Inspection Scope

The inspectors reviewed the condition reports (CR) listed below which documented

equipment problems to: (1) verify the appropriate handling of structure, system, and

component (SSC) performance or condition problems; (2) verify the appropriate

handling of degraded SSC functional performance; (3) evaluate the role of work

practices and common cause problems; and (4) evaluate the handling of SSC issues

reviewed under the requirements of the maintenance rule; 10 CFR Part 50, Appendix B;

and TS.

on June 2, 2006, and CR-RBS-2004-4338, main steam stop Valve B21-

MOVF098C high leakage during RFO-11 and -12, reviewed on June 26, 2006.

functional failure, reviewed on June 26, 2006.

Documents reviewed by the inspectors included:

  • NUMARC 93-01, Nuclear Energy Institute Industry (NEI) Guideline for Monitoring

the Effectiveness of Maintenance at Nuclear Power Plants, Revision 2

  • Maintenance rule function list
  • Maintenance rule performance criteria list
  • Main steam stop valve maintenance rule performance evaluations

The inspectors completed two inspection samples.

b. Findings

No findings of significance were identified.

1R13 Maintenance Risk Assessments and Emergent Work Control

a. Inspection Scope

.1 Risk Assessment and Management of Risk

The inspectors reviewed the planned work weeks listed below to verify: (1) that the

licensee performed risk assessments when required by 10 CFR 50.65 (a)(4) and

administrative Procedure ADM-096, Risk Management Program Implementation and

On-Line Maintenance Risk Assessment, Revision 4B, prior to changes in plant

configuration for maintenance activities and plant operations; (2) the accuracy,

adequacy, and completeness of the information considered in the risk assessment;

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(3) that the licensee recognized, and entered as applicable, the appropriate licensee

established risk category according to the risk assessment results and Procedure ADM-

096; and (4) that the licensee identified and corrected problems related to maintenance

risk assessments. Specific work activities evaluated included planned and emergent

work for the weeks of:

  • June 5, 2006, Division I work week and preferred station service Transformer

RTX-ESR1F cooling oil dehydration

  • June 19, 2006, planned Division II EDG outage week
  • June 26, 2006, nondivisional work week and potential labor work stoppage

.2 Emergent Work Control

For the two emergent work activities listed below, the inspectors: (1) verified that the

licensee performed actions to minimize the probability of initiating events and

maintained the functional capability of mitigating systems and barrier integrity systems;

(2) verified that emergent work related activities such as troubleshooting, work

planning/scheduling, establishing plant conditions, aligning equipment, tagging,

temporary modifications, and equipment restoration did not place the plant in an

unacceptable configuration; and (3) reviewed the CAP to determine if the licensee

identified and corrected risk assessment and emergent work control problems.

  • Preferred station service Transformer RTX-ESR1F sudden pressure relay failure

on May 30, 2006

The inspectors completed five inspection samples.

c. Findings

No findings of significance were identified.

1R14 Operator Performance During Nonroutine Evolutions and Events

a. Inspection Scope

1. April 4, 2006, Automatic Initiation of Standby Service Water

The inspectors: (1) reviewed operator logs, plant computer data, and strip charts for the

April 4, 2006, unexpected initiation of Division II standby service water that occurred

while swapping the running normal service water pumps to evaluate operator

performance in coping with the event; (2) verified that operator actions were in

accordance with the response required by plant procedures and training; and (3) verified

that the licensee identified and implemented appropriate corrective actions associated

with personnel performance problems that occurred during the transient. In addition, the

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inspectors reviewed CR-RBS-2006-01257, which documented the procedural problems

that led to the event and reviewed the following procedures used by the operators:

Running, Revision 8

  • SOP-66, Control Building HVAC Chilled Water System, Revision 33B

2. April 15, 2006, Reactor Scram

The inspectors: (1) reviewed operator logs, plant computer data, and strip charts for the

April 15, 2006, unexpected reactor recirculation pump downshift and subsequent reactor

scram to evaluate operator performance in coping with the event; (2) verified that

operator actions were in accordance with the response required by plant procedures

and training; and (3) verified that the licensee identified and implemented appropriate

corrective actions associated with personnel performance problems that occurred during

the transient. In addition the inspectors reviewed the postscram report documented in

Procedure GOP-003, Scram Recovery, Revision 16A, and observed the onsite safety

review committee review of the postscram report.

The inspectors completed two inspection samples.

e. Findings

No findings of significance were identified.

1R15 Operability Evaluations

a. Inspection Scope

For the operability evaluations associated with the documents listed below, the

inspectors: (1) reviewed plants status documents such as operator shift logs, emergent

work documentation, deferred modifications, and standing orders, to determine if an

operability evaluation was warranted for degraded components; (2) referred to the

USAR and design basis documents to review the technical adequacy of licensee

operability evaluations; (3) evaluated compensatory measures associated with

operability evaluations; (4) determined degraded component impact on any TS; (5) used

the significance determination process to evaluate the risk significance of degraded or

inoperable equipment; and (6) verified that the licensee identified and implemented

appropriate corrective actions associated with degraded components.

to meet leak rate acceptance criteria, reviewed during the week of April 3, 2006

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calculation revised for extended operating cycle, reviewed during the week of

April 17, 2006

  • Work Request (WR) 76625, NNS-ACB23 control power light out, suspect bad

socket, reviewed during the week of May 29, 2006

  • TS-LCO-06-0711, Division II EDG Generator Output Breaker charging springs

did not charge during tagout restoration, reviewed on June 23, 2006

pressure, reviewed on June 28, 2006

June 28, 2006

Other documents reviewed by the inspectors are listed in the attachment.

The inspectors completed six inspection samples.

b. Findings

Introduction: The inspectors reviewed a self-revealing noncited violation (NCV) of

10 CFR Part 50, Appendix B, Criterion XVI, "Corrective Action," involving the failure of

the licensee to identify that the normal supply breaker to the Division III 4.16 kV

engineered safety features (ESF) bus was not properly racked in following maintenance.

Description: Following the completion of planned maintenance on Switchgear NNS-

SWG1A on April 29, 2006, operators were assigned to clear equipment tags and restore

the system alignment. As part of this task, operators racked in Breaker NNS-ACB23,

the normal supply breaker to 4.16 kV Switchgear NNS-SWG1C. No actions, such as

cycling the breaker, were required to verify that the breaker was properly racked in.

On May 9, 2006, after noting that the control power light associated with Breaker NNS-

ACB23 was not lit, operators wrote WR 76625 to repair the light. The WR stated that

the white control power light on Control Room Panel H13-P808 was out with the breaker

racked in and the control power fuses installed. The WR also indicated that the

suspected cause was a bad socket and that position Switch 52H had failed in the past to

make up during closure. A work control center senior reactor operator determined that

an operability evaluation was not required for the condition described in WR 76625. The

WR was classified 4D, which indicated that it should be scheduled as resources

allowed within the normal 16-week work planning schedule. The inspectors noted the

licensee did not write a CR. The white control power light provides indication that the

breaker is functional, specifically, that: (1) there is no electrical fault on the line or load

side of the breaker, (2) the breaker Lockout button is not depressed on Panel 808, and

(3) the breaker is fully racked into the switchgear. On May 9, 2006, there were no

electrical faults on Breaker NNS-ACB23 and the Lockout was reset on Panel 808.

-13- Enclosure

On May 22, 2006, while aligning Switchgear NNS-SWG1C and the Division III 4.16 kV

ESF bus to the Transformer RSS1 offsite power supply, Breaker NNS-ACB23 failed to

close. Operators racked the breaker out and in, but the breaker failed to close on the

second attempt. Subsequent troubleshooting identified that the breaker had not been

fully racked in as electricians were able to rotate the racking device one additional turn.

The white light on Panel 808 came on and the breaker was successfully closed. The

operators and electricians determined that Breaker NNS-ACB23 had not been not

properly racked in, wrote CR-RBS-2006-02325 and -02337 and initiated WR 77478 to

investigate the problem with racking in Breaker NNS-ACB23.

On May 25, 2006, the inspectors questioned the impact that the failure of the breaker to

close had on the licensees compliance with TS. Specifically, TS 3.8.1.a requires two

qualified circuits between the offsite transmission network and the onsite Class 1E ac

electrical power distribution system when the plant is in Modes 1, 2, and 3. On May 12,

the plant was taken from Mode 4 to Mode 2 without two qualified offsite power sources

available to the Division III 4.16 kV ESF bus. The licensee wrote CR-RBS-2006-2402

and determined that they did not comply with TS 3.8.1.a when they changed modes on

May 12. In addition, the Division III 4.16 kV ESF bus was inoperable for a period of

10 days (May 12-22), which exceeded the allowed outage time of 72 hours8.333333e-4 days <br />0.02 hours <br />1.190476e-4 weeks <br />2.7396e-5 months <br /> specified in

TS Condition 3.8.1.A. The licensee also discovered that, on May 14 during the conduct

of maintenance on the Division I EDG, with Breaker NNS-ACB23 unable to be closed,

they unknowingly entered TS Condition 3.8.1.d. TS Condition 3.8.1.d states that with

One required offsite circuit inoperable AND on required [E]DG inoperable, restore the

EDG or the offsite power supply to an operable status in 12 hours1.388889e-4 days <br />0.00333 hours <br />1.984127e-5 weeks <br />4.566e-6 months <br /> or place the plant in

Mode 3 within the next 12 hours1.388889e-4 days <br />0.00333 hours <br />1.984127e-5 weeks <br />4.566e-6 months <br />. The Division I EDG was inoperable for 15 hours1.736111e-4 days <br />0.00417 hours <br />2.480159e-5 weeks <br />5.7075e-6 months <br /> and

15 minutes.

The inspectors found that the licensees procedures did not require Breaker NNS-

ACB23 to be cycled to verify proper operation after it was racked in on April 29.

Procedure OSP-0022, Operations General Administrative Guidelines, Revision 01,

step 4.5.5, required that breakers be functionally tested following any activity involving

safety related equipment which requires the breaker to be racked out. Because

Breaker NNS-ACB23 is not classified as a safety-related breaker, it was not required to

be functionally tested after it was racked in on April 29.

Analysis: The performance deficiency associated with this finding involved the failure of

operators to identify that Breaker NNS-ACB23 was not functional on April 29, 2006. The

finding was more than minor because it was associated with the mitigating system

cornerstone attribute of configuration control and affected the associated cornerstone

objective to ensure the availability, reliability, and capability of systems that respond to

initiating events to prevent undesirable consequences. The Phase 1 worksheets in

Manual Chapter (MC) 0609, "Significance Determination Process," were used to

conclude that a Phase 2 analysis was required because both the mitigating systems and

the containment barrier cornerstones were affected.

In accordance with NRC Inspection Manual Chapter 0609, Appendix A, Attachment 1,

"User Guidance for Determining the Significance of Reactor Inspection Findings for

At-Power Situations," the inspectors estimated the risk of the subject finding using the

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Risk-Informed Inspection Notebook for River Bend Station, Revision 2. The inspectors

assumed that Division III power was available, but degraded, while Breaker NNS-ACB23

was not properly installed for the 10 days that the plant was in Mode 3 or above, from

May 12-22, 2006. Therefore, the exposure window used was 3-30 days. No operator

recovery was credited because on two occasions, operators had proven incapable of

properly positioning the breaker, ultimately requiring maintenance technicians to

properly install the breaker. Using Manual Chapter 0609, Appendix A, Attachment 2,

Rule 2.1, Inspection Finding that Degrades Mitigation Capability and Does Not Reduce

Remaining Mitigation Capability Credit to a Value Less Than Full Mitigation Credit, the

inspectors determined that all sequences containing the functions that would be affected

by a loss of Division III power, including the Division I standby service water loop

(HPCS, LPI, CHR, HPCS/LC, and REC/SSW), should be quantified, giving full mitigation

capability credit to each of these functions. Because the performance deficiency

affected the electric power system, Table 2 of the risk-informed notebook required that

all worksheets be evaluated. The resulting dominant sequences are provided in Table 1

below:

Table 1

Phase 2 Worksheet Results

Initiator Sequence IEL Mitigating Functions Result

TNSW 5 3 SSW - REC/SSW 7*

4 3 RCIC - HPCS - DEP 9*

1 3 CHR - LDEP 8

2 3 CHR - SPCFAN 8

LOOP 4 3 RCIC - HPCS - DEP 9*

6 3 EAC1&2 - HPCS - REC6 - FPW 9*

8 3 EAC1&2 - HPCS - SBODG - REC4 9*

9 3 EAC1&2 - REC1 - HPCS -RCIC 9*

1 3 CHR-LDEP 8

SORV 2 3 CHR - SPCFAN 9

4 3 RCIC - HPCS - DEP 9*

2 4 CHR - SPCFAN 8

LOIA

1 4 CHR-LDEP 9

TPCS 4 2 RCIC - HPCS - DEP 8

ATWS 1 6 CHR 9

  • Denotes sequences indicated as LERF contributors in the Phase 2 notebook.

By application of the counting rule, the internal event risk contribution of this finding to

the change in core damage frequency (CDF) was determined to be of low to moderate

risk significance (WHITE).

A senior reactor analyst performed further evaluation of the risk associated with this

issue (Phase 3/Modified Phase 2). Because the assumptions made during the Phase 2

estimation process were overly conservative and did not completely represent the actual

exposure time nor the actual affect the performance deficiency had on the availability of

power to the Division III diesel generator, the senior reactor analyst modified these

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assumptions to more precisely quantify the change in risk. Specifically, the exposure

time was 10 days as opposed to the 30 days used in the risk-informed notebook.

Additionally, the Phase 2 evaluation included loss of offsite power initiating events that

were not affected by the performance deficiency because offsite power to Division III

would in all likelihood be lost during a design basis loss of offsite power. The senior

reactor analyst performed a modified Phase 2 estimation and determined that the

internal event risk contribution of the subject finding to the CDF was of very low risk

significance (Green). The best estimate value of this probability (CDFINTERNAL) was

calculated by the senior reactor analyst to be 1.2 x 10-7. The analyst evaluated the

contribution of external initiating events to the risk and calculated a bounding risk

estimate of 2.9 x 10-7 as the CDF for internal fire events.

Using Manual Chapter 0609, Appendix H, Containment Integrity Significance

Determination Process, the analyst estimated that the potential risk contribution from

large early release frequency was 6.6 x 10-8.

Given the independence of each initiating event, the analyst determined that the best

estimate of the total risk related to the subject performance deficiency was the

summation of the CDF calculated for both internal and external initiators. Therefore,

the best estimate was 4.1 x 10-7. The change in risk related to large early release

frequency was determined to be below 6.6 x 10-8, corroborating that the finding was of

very low risk significance. The performance deficiency resulted in a finding that was of

very low risk significance (Green). The cause of the finding was related to the

crosscutting aspect of problem identification and resolution in that operators failed to

identify that Breaker NNS-ACB23 was not properly racked in.

Enforcement: 10 CFR Part 50, Appendix B, Criterion XVI, Corrective Action, requires, in

part, that measures be established to assure that conditions adverse to quality are

promptly identified and corrected. Contrary to this, from April 29 to May 22, 2006, the

licensee failed to identify that Breaker NNS-ACB23, which supplied one of the two

required offsite power supplies to the Division III 4.16 kV ESF bus, was not properly

racked in to Switchgear NNS-SWGIC. The root cause involved the licensees lack of

understanding that Breaker NNS-ACB23 was required to be functional to meet

TS 3.8.1.a requirements for two offsite power circuits to the Division III 4.16 kV ESF

bus. The corrective actions to restore compliance included: (1) changes to operations

section procedures to verify the white control power light, when applicable, after a circuit

breaker is racked in, (2) expansion of the requirement to functionally test safety-related

breakers to the nonsafety-related breakers in the TS required offsite power circuits, and

(3) operator lessons learned training on the event and all of its ramifications. Because

the finding was of very low safety significance and has been entered into the licensees

CAP as CR-RBS-2006-02402, this violation is being treated as an NCV consistent with

Section VI.A of the Enforcement Policy: NCV 05000458/2006003-01, Failure to identify

Division III ESF bus supply breaker not racked in.

-16- Enclosure

1R19 Postmaintenance Testing

a. Inspection Scope

For the five postmaintenance test activities of risk significant systems or components

listed below, the inspectors: (1) reviewed the applicable licensing basis and/or design-

basis documents to determine the safety functions; (2) evaluated the safety functions

that may have been affected by the maintenance activity; and (3) reviewed the test

procedure to verify that it adequately tested the safety function that may have been

affected. The inspectors either witnessed or reviewed test data to verify that

acceptance criteria were met, plant impacts were evaluated, test equipment was

calibrated, procedures were followed, jumpers were properly controlled, the test data

results were complete and accurate, the test equipment was removed, the system was

properly re-aligned, and deficiencies during testing were documented. The inspectors

also reviewed the CAP to determine if the licensee identified and corrected problems

related to postmaintenance testing.

  • Work Order (WO) 50370422, Division II battery cell post seal replacement,

reviewed during the week of May 8, 2006

scram test switches, reviewed May 19, 2006

VF033 replacement, reviewed during the week of June 19, 2006

service water outlet valve, SWP-MOV74B, reviewed during the week of June 19,

2006

  • WO 90342, Division II EDG generator output Breaker ENS-SWG1B-ACB027

charging springs failed to charge during tagout restoration, reviewed on June 23,

2006

The inspectors completed five inspection samples.

g. Findings

No findings of significance were identified.

1R20 Refueling and Other Outage Activities

a. Inspection Scope

The inspectors reviewed the following risk important refueling outage activities to verify

defense in depth commensurate with the outage risk control plan and compliance with

the TS during RFO-13 from April 23 to May 12, 2006: (1) the risk control plan;

(2) tagging/clearance activities; (3) reactor coolant system instrumentation; (4) electrical

-17- Enclosure

power; (5) decay heat removal; (6) spent fuel pool cooling; (7) inventory control;

(8) reactivity control; (9) containment closure; (10) reduced inventory conditions;

(11) refueling activities; (12) heatup and cooldown activities; (13) restart activities; and

(14) licensee identification and implementation of appropriate corrective actions

associated with RFO activities. The inspectors' containment inspections included

observations of the containment sump for damage and debris, and supports, braces,

and snubbers for evidence of excessive stress, water hammer, or aging. Specific

outage activities observed and reviewed included:

  • Outage risk assessment team (ORAT) report to onsite safety review committee
  • Reactor shutdown, cooldown, and vessel disassembly
  • Refueling operations, fuel sipping, and off loaded fuel inspections
  • Daily/shiftly shutdown operations protection plan assessments
  • Shutdown postscram report to onsite safety review committee
  • Transformer RSS1 offsite power line equipment inspection and upgrade
  • Division II to Division I protected division swap
  • Infrequently performed test or evolution briefings for:

- Divisional loss of offsite power/loss of coolant accident testing

- Concurrent control rod mechanism and blade changeout

- Reactor vessel pressure test and scram time testing

- Reactor startup, heatup, and power ascension

- Onsite safety review committee meeting to recommend startup

- Drywell 900 psi walkdown (after shutdown and during startup)

Documents reviewed by the inspectors are listed in the attachment.

The inspectors completed one inspection sample.

b. Findings

Introduction: An NRC identified NCV of 10 CFR 50.65, Maintenance Rule,

Section (a)(4) was identified for the failure of the licensee to provide prescribed

compensatory measures for the highest shutdown risk condition during RFO-13.

Specifically, the preoutage risk assessment recommended that two WOs be in place for

maintenance electricians to provide power to one spent fuel pool cooling pump in the

event of problems with the running pump during periods of safety-related electrical bus

maintenance. The inspectors found that the WOs were not in place before entering

shutdown risk condition Orange on April 26, 2006, during the Division II ESF bus testing,

and on May 3, 2006, during the Division I ESF bus outage.

Description: The inspectors observed the onsite safety review committee meeting to

discuss and approve the ORAT report for RFO-13. The report noted two Orange

shutdown risk conditions for spent fuel pool cooling (SFC). Only one SFC pump would

be available after the beginning of core offload: (1) during the Division II ESF bus

testing with the SFC-P1B breaker racked out, and (2) during the Division I ESF bus

outage when SFC-P1A was without power. As a result of the ORAT review of

-18- Enclosure

Procedure AOP-0051, Loss of Decay Heat Removal, Revision 17, they recommended

that the planned maintenance optimization group develop WOs for maintenance

electricians to provide alternate power from the station blackout diesel generator to the

deenergized SFC pump in the event of a failure of the running pump.

In addition, Procedure OSP-0037, Shutdown Operations Protection Plan, Revision 16,

Section 4.7, Fuel Pool Cooling, required that: (1) if work was required on SFC during

the outage, then it should be done as early as possible in the outage and not after fuel

offload (when heat load is the highest); and (2) if work was required after fuel offload,

then a contingency plan shall be in place prior to removing the system from service.

The inspectors determined that this requirement applied to deenergizing an SFC pump

for electrical bus maintenance.

On May 3, 2006, during the Division I ESF bus outage, the inspectors asked the

operations shift manager if the required WO was available to provide alternate power to

SFC-P1A in the event that the running SFC-P1B failed. He stated that he assumed that

the WO was written and that he would check. The inspectors then requested a copy of

the WO and a senior work planner reported that the WO was not available since it was

not yet approved for use in the electronic work planning program. Following discussions

with operators in the work management center, the licensee immediately took actions to

ensure that both WOs were processed and made ready for use.

The inspectors reviewed AOP-0051, Attachment 1, Spent Fuel Pool Curves, and

determined that the approximate time to boil for the spent fuel pool at that time with

offload fuel in the pool was approximately 8 hours9.259259e-5 days <br />0.00222 hours <br />1.322751e-5 weeks <br />3.044e-6 months <br />. Based on that data and the time

needed to generate the WOs, the inspectors determined that there was adequate time

for the licensee to connect an alternate power supply to the SFC pumps before the

spent fuel pool water started to boil if there was a failure of the running pump.

Analysis: The performance deficiency associated with this finding involved the failure to

establish prescribed compensatory measures for the highest outage risk condition

during RFO-13 as required by the shutdown operations protection plan. The finding was

more than minor because the licensee failed to implement prescribed compensatory

measures and failed to effectively manage those measures. The finding affected the

mitigating system cornerstone because of the increased risk of a sustained loss of SFC

during core offloading operations. The finding could not be evaluated using the

significance determination process; therefore, the finding was reviewed by regional

management and determined to be of very low safety significance. Factors that were

considered included: (1) electrical maintenance technicians had previously performed

the task of providing alternate power to an SFC pump, (2) the necessary equipment was

staged as part of the abnormal operating procedure for loss of decay heat removal, and

(3) the relatively long time to boil of the spent fuel storage pool at that time during the

refueling outage. The cause of the finding was related to the crosscutting aspect of

human performance because the licensees planned maintenance activities and the

predetermined increase in outage risk was not effectively managed by prescribed

compensatory measures.

-19- Enclosure

Enforcement: 10 CFR 50.65(a)(4) requires, in part, that before performing maintenance

activities, the licensee shall assess and manage the increase in risk that may result from

the proposed maintenance activities. Contrary to this, the licensee failed to properly

manage the highest outage risk condition of RFO-13. On April 26, 2006, the plant

entered an Orange outage risk condition for SFC during core offload, when SFC-P1B

was deenergized for Division II ESF bus testing. On May 3, 2006, the plant entered an

Orange outage risk condition for SFC during core offload, when SFC-P1A was

deenergized for a Division I ESF bus outage. WOs were not written and ready for use

to have electricians provide alternate power to an SFC pump in the event the running

pump failed. The root cause involved the failure of the licensee to ensure that the WO

was in place before the plant entered the Orange shutdown risk condition. Corrective

action was taken to process the WOs for immediate use. Because the finding was of

very low safety significance and was entered into the licensees CAP as CR-RBS-2006-

01937, this violation is being treated as an NCV consistent with Section VI.A of the

Enforcement Policy: NCV 05000458/2006003-02, "Failure to adequately manage an

increase in plant risk."

1R22 Surveillance Testing

a. Inspection Scope

The inspectors reviewed the USAR, procedure requirements, and TS to ensure that the

six surveillance activities listed below demonstrated that the SSCs tested were capable

of performing their intended safety functions. The inspectors either witnessed or

reviewed test data to verify that the following significant surveillance test attributes were

adequate: (1) preconditioning; (2) evaluation of testing impact on the plant;

(3) acceptance criteria; (4) test equipment; (5) procedures; (6) jumper/lifted lead

controls; (7) test data; (8) testing frequency and method demonstrated TS operability;

(9) test equipment removal; (10) restoration of plant systems; (11) fulfillment of ASME

Code requirements; (12) updating of performance indicator (PI) data; (13) engineering

evaluations, root causes, and bases for returning tested SSCs not meeting the test

acceptance criteria were correct; (14) reference setting data; and (15) annunciator and

alarm setpoints. The inspectors also verified that the licensee identified and

implemented any needed corrective actions associated with the surveillance testing.

Rate Test and Inboard MSIV Inleakage Test," Revision 6, performed on May 2,

2006

  • STP-305-1606, [Division I Battery] ENB-BAT1A Service Discharge Test,

Revision 17, performed on May 6, 2006

May 12, 2006

  • STP-000-0102, Power Distribution Alignment Check, Revision 5, performed on

May 14 and 15, 2006

-20- Enclosure

  • STP-508-4543, Turbine First Stage Pressure Channel Functional Test,

Revision 7, performed on June 4, 2006

Balance-Of-Plant Systems, Attachment 8, Reactor Sample Panel Routine

Sample Points, Revision 14, and COP-0305, Operation of the Countroom

Analysis Systems, Revision 2, performed on June 15, 2006

Documents reviewed by the inspectors are listed in the attachment.

The inspectors completed six inspection samples.

h. Findings

Introduction: The inspectors identified an NCV of TS 5.4.1.a for the failure of the

licensee to provide an adequate surveillance test procedure to perform TS Surveillance

Requirement (SR) 3.8.1.1. Specifically, STP-000-0102, Power Distribution Alignment

Check, Revision 4, did not include steps to verify the required offsite power circuit

breaker alignment and indicated power availability for the Division III 4.16 kV ESF bus

as required in Modes 1, 2, and 3.

Description: As discussed in Section 1R15 of this report, operators failed to properly

rack in Breaker NNS-ACB23 on April 29, 2006. This condition was discovered on

May 22, when the breaker failed to close. During this period, on May 14, 2006, the

Division I EDG was removed from service to replace a leaking section of jacket cooling

water vent tubing. With the Division I EDG removed from service, TS Required

Action 3.8.1.a.1 required that operators perform TS SR 3.8.1.1 within one hour and

once every 8 hours9.259259e-5 days <br />0.00222 hours <br />1.322751e-5 weeks <br />3.044e-6 months <br /> until the EDG was operable. TS SR 3.8.1.1 required operators to

verify the correct breaker alignment and indicated power for each required offsite power

circuit. Operators utilized Procedure STP-000-0102, Power Distribution Alignment

Check, Revision 4, to satisfy the requirements of TS SR 3.8.1.1; however, the

inspectors identified that the procedure did not have steps to verify the correct breaker

alignment and indicated power availability to the Division III 4.16 kV ESF bus. As a

result, the operators did not identify that Breaker NNS-ACB23 was not racked in.

During the period that the Division I EDG was removed from service, the plant was

actually in TS Condition 3.8.1.d. TS Condition 3.8.1.d states that with One required

offsite circuit inoperable AND one required [E]DG inoperable, restore the EDG or the

offsite power supply to an operable status in 12 hours1.388889e-4 days <br />0.00333 hours <br />1.984127e-5 weeks <br />4.566e-6 months <br /> or place the plant in Mode 3 within

the next 12 hours1.388889e-4 days <br />0.00333 hours <br />1.984127e-5 weeks <br />4.566e-6 months <br />. The Division I EDG was inoperable for 15 hours1.736111e-4 days <br />0.00417 hours <br />2.480159e-5 weeks <br />5.7075e-6 months <br /> and 15 minutes.

Procedure STP-000-0102, Section 1.1, states, in part, that its purpose is to verify the

correct breaker alignment and indicated power availability for each required offsite

power circuit in accordance with TS SR 3.8.1.1 in Modes 1, 2, and 3. TS 3.8.1 bases

defines an offsite power circuit as follows: Each offsite circuit consists of incoming

breakers and disconnects to the respective preferred station service Transformers 1C

and 1D [RSS1 and RSS2], the 1C and 1D preferred station service transformers, and

the respective circuit path including feeder breakers to the three 4.16 kV ESF buses.

-21- Enclosure

NNS-ACB23 is one of the circuit breakers between preferred station service

Transformer RTX-XSR1C and the Division III 4.16 kV ESF bus.

Analysis: The performance deficiency associated with this finding involved the

licensees failure to provide operators with an adequate STP to meet the requirements

of TS SR 3.8.1.1 to verify correct breaker alignment and indicated power availability to

the Division III ESF bus for each required offsite circuit. A review of previous revisions

of STP-000-0102 showed that the procedure has never verified the required offsite

power circuits for the Division III 4.16 kV ESF bus in Modes 1, 2, and 3. Although this

performance deficiency caused the failure to verify the offsite power circuit for an

extended period of time, the risk impact was limited to the 10 days from May 12-22,

2006. Therefore, the risk characterization of this finding is the same as that described in

Section 1R15 of this inspection report. The cause of the finding was related to the

crosscutting aspect of human performance because the licensee did not provide the

operators with an adequate STP to complete the TS SR to verify the required offsite

power circuits breaker alignment to all three 4.16 kV ESF buses. Additionally, the

cause of the finding was related to the crosscutting aspect of problem identification and

resolution in that on two occasions, June 18, 2005, and May 22, 2006, operators

entered TS Condition 3.8.1.a for one inoperable offsite power circuit to the Division III

4.16 kV ESF bus and performed STP-000-0102 to meet the Required Action to perform

SR 3.8.1.1, but did not recognize that STP-000-0102 did not verify the other offsite

power circuit breaker alignment to the Division III 4.16 kV ESF bus.

Enforcement: TS 5.4.1.a requires that written procedures be established, implemented,

and maintained covering the activities specified in Appendix A, "Typical Procedures for

Pressurized Water Reactors and Boiling Water Reactors," of Regulatory Guide 1.33,

"Quality Assurance Program Requirements (Operation)," dated February 1978.

Regulatory Guide 1.33, Appendix A, Section 8.a, requires procedures for all TS SRs.

Procedure STP-000-0102 states that it verified the correct breaker alignment and power

availability for each required offsite circuit in accordance with TS SR 3.8.1.1 in Modes 1,

2, and 3. Contrary to this, Procedure STP-000-0102, Revision 4, did not require

verification of the correct breaker alignment for the offsite power circuits to the

Division III 4.16 kV ESF bus in Modes 1, 2, and 3. The root cause involved the incorrect

interpretation of the Division III 4.16 kV bus SRs as they apply to the unique River Bend

Station ESF electrical distribution system. The corrective actions to restore compliance

included as an interim measure entering in the control room logs the breaker alignment

for and the bus voltage available to the Division III 4.16 kV ESF bus, until STP-000-0102

could be revised. Because the finding was of very low safety significance and has been

entered into the licensees CAP as CR-RBS-2006-02675 and -02402, this violation is

being treated as an NCV consistent with Section VI.A of the Enforcement Policy: NCV 05000458/2006003-03, Inadequate procedure to verify required offsite power breaker

alignment.

-22- Enclosure

1R23 Temporary Plant Modifications

a. Inspection Scope

The inspectors reviewed the USAR, plant drawings, procedure requirements, and TS to

ensure that Temporary Alteration 2006-0011, Off Gas Pretreatment Radiation Monitor

Sample Chamber Drain Line Modification, was properly implemented. The inspectors:

(1) verified that the modification did not have an affect on system operability/availability;

(2) verified that the installation was consistent with modification documents; (3) ensured

that the postinstallation test results were satisfactory and that the impact of the

temporary modification on the operation of the pretreatment radiation monitor were

supported by the test; (4) verified that the modification was identified on control room

drawings and that appropriate identification tags were placed on the affected drawings;

and (5) verified that appropriate safety evaluations were completed. The inspectors

verified that the licensee identified and implemented any needed corrective actions

associated with temporary modifications.

The inspectors completed one inspection sample.

b. Findings

No findings of significance were identified.

Cornerstone: Emergency Preparedness

1EP6 Drill Evaluation

a. Inspection Scope

On June 20, 2006, the inspectors observed the full scope exercise dress rehearsal,

which was used to contribute to Drill/Exercise Performance and Emergency Response

Organization Drill Performance PI. The inspectors: (1) observed the training evolution

to identify any weaknesses and deficiencies in classification, notification, and protective

action requirements development activities; (2) compared the identified weaknesses and

deficiencies against licensee identified findings to determine whether the licensee was

properly identifying failures; and (3) determined whether licensee performance was in

accordance with the guidance of the NEI 99-02, "Voluntary Submission of Performance

Indicator Data," Revision 2, acceptance criteria. The scenario used was RDRL-EP-

0602, Tornado/Loss of Offsite Power/Main Steam Line Break, dated June 16, 2006.

Emergency [plan] implementing procedures reviewed by the inspectors included:

  • EIP-2-001, Classification of Emergencies, Revision 13
  • EIP-2-006, Notifications, Revision 32
  • EIP-2-007, Protective Action Guidelines Recommendations, Revision 21

The inspectors completed one inspection sample.

-23- Enclosure

b. Findings

No findings of significance were identified.

2. RADIATION SAFETY

Cornerstone: Occupational Radiation Safety

2OS1 Access Control to Radiologically Significant Areas

a. Inspection Scope

This area was inspected to assess the licensees performance in implementing physical

and administrative controls for airborne radioactivity areas, radiation areas, high

radiation areas, and worker adherence to these controls. The inspector used the

requirements in 10 CFR Part 20, TS, and the licensees procedures required by TS as

criteria for determining compliance. During the inspection, the inspector interviewed the

radiation protection manager, radiation protection supervisors, and radiation workers.

The inspector performed independent radiation dose rate measurements and reviewed

the following items:

  • PI events and associated documentation packages reported by the licensee in

the occupational radiation safety cornerstone

  • Controls (surveys, posting, and barricades) of three radiation, high radiation, or

airborne radioactivity areas

  • Radiation work permits, procedures, engineering controls, and air sampler

locations

  • Conformation of electronic personal dosimeter alarm setpoints with survey

indications and plant policy; workers knowledge of required actions when their

electronic personnel dosimeter noticeably malfunctions or alarms

areas

  • Adequacy of the licensees internal dose assessment for any actual internal

exposure greater than 50 millirem committed effective dose equivalent

  • Physical and programmatic controls for highly activated or contaminated

materials (nonfuel) stored within spent fuel and other storage pools.

  • Self-assessments, audits, licensee event reports (LER), and special reports

related to the access control program since the last inspection

  • Corrective action documents related to access controls

-24- Enclosure

  • Licensee actions in cases of repetitive deficiencies or significant individual

deficiencies

  • Radiation work permit briefings and worker instructions
  • Adequacy of radiological controls, such as required surveys, radiation protection

job coverage, and contamination controls during job performance

  • Dosimetry placement in high radiation work areas with significant dose rate

gradients

and very high radiation areas

  • Controls for special areas that have the potential to become very high radiation

areas during certain plant operations

  • Posting and locking of entrances to all accessible high dose rate - high radiation

areas and very high radiation areas

  • Radiation worker and radiation protection technician performance with respect to

radiation protection work requirements

The inspector completed 21 of the required 21 samples.

b. Findings

1. Unguarded High Radiation Area Boundary

Introduction: The inspector reviewed a self-revealing NCV of TS 5.7.1, resulting from

the licensees failure to control access to a high radiation area. The finding had very low

safety significance.

Description: On April 6, 2006, the licensee transferred reverse osmosis system filters

from one elevation of the radwaste building to another. Because dose rates on the filter

barrels were as high as 600 millirem per hour, the licensee assigned personnel to guard

the elevator entrances to prevent workers from entering high radiation areas. On this

occasion, the guards were not using radios, as was a common practice. Because of the

lack of good communication, a guard prematurely left his post in front of the 123-foot

elevation elevator door. Coincidently, two workers attempted to board the elevator on

the 123-foot elevation after the guard had left. The elevator carrying the barrels of

radioactive filters stopped at the 123-foot elevation, the doors opened, and the

electronic dosimeters of the workers alarmed because of the high dose rates. The

guard returned and evacuated the workers before they accrued additional radiation

dose. The highest dose rate recorded by an electronic alarming dosimeter was 164

millirem per hour. Planned corrective action was still being evaluated by the licensee at

the conclusion of the inspection.

-25- Enclosure

Analysis: The failure to control access to a high radiation area was a performance

deficiency. The significance of the finding was greater than minor because it was

associated with the occupational radiation safety attribute of exposure control and

affected the cornerstone objective, in that not controlling access to a high radiation area

could increase personal exposure. Using the Occupational Radiation Safety

Significance Determination Process, the inspector determined that the finding was of

very low safety significance because it did not involve: (1) an as low as is reasonably

achievable (ALARA) finding, (2) an overexposure, (3) a substantial potential for

overexposure, or (4) an impaired ability to assess dose. Additionally, this finding had

crosscutting aspects associated with human performance in that the failure of the

individual to guard the elevator door directly contributed to the violation.

Enforcement: TS 5.7.1 requires each high radiation area, as defined in 10 CFR Part 20,

in which the intensity of radiation is greater than 100 millirems per hour but less than

1000 millirems per hour, be barricaded and conspicuously posted as a high radiation

area and entrance thereto shall be controlled by requiring issuance of a radiation work

permit. The licensee violated TS 5.7.1 when it failed to barricade and conspicuously

post the elevator housing the radioactive filter barrels or maintain a guard to ensure

workers did not enter a high radiation area. Because this failure to control a high

radiation area was of very low safety significance and has been entered into the

licensees CAP as CR-RBS-2006-01294, this violation is being treated as an NCV,

consistent with Section VI.A of the NRC Enforcement Policy:

NCV 05000458/2006003-04, Failure to control access to a high radiation area.

2. Unanalyzed Airborne Radioactivity Survey

Introduction: The inspector identified an NCV of 10 CFR 20.1501(a) because the

licensee failed to survey airborne radioactivity. The finding had very low significance.

Description: On May 2, 2006, during the removal of local power range monitors, the

licensee started collecting an air sample of the work area. The air sample spanned two

shifts. A health physics technician on the second shift discarded the sample because

the first shift had not documented a start time. Therefore, the sample was never

analyzed. However, all workers successfully passed through the portal monitors at the

exit of the controlled access area without alarm, confirming that no worker experienced

an uptake of radioactive material. Planned corrective action is still being evaluated.

Analysis: The failure to survey airborne radioactivity was a performance deficiency.

This finding was greater than minor because it was associated with the occupational

radiation safety program attribute of exposure control and affected the cornerstone

objective in that the lack of knowledge of radiological conditions could increase

personnel dose. Using the Occupational Radiation Safety Significance Determination

Process, the inspector determined that the finding was of very low safety significance

because it did not involve: (1) an ALARA finding, (2) an overexposure, (3) a substantial

potential for overexposure, or (4) an impaired ability to assess dose. Additionally, this

finding had crosscutting aspects associated with human performance in that the failure

to maintain the sample for analysis directly contributed to the violation.

-26- Enclosure

Enforcement: 10 CFR 20.1501(a) requires that each licensee make or cause to be

made surveys that may be necessary for the licensee to comply with the regulations in

10 CFR Part 20 and that are reasonable under the circumstances to evaluate the extent

of radiation levels, concentrations or quantities of radioactive materials, and the potential

radiological hazards that could be present. Pursuant to 10 CFR 20.1003, a survey

means an evaluation of the radiological conditions and potential hazards incident to the

production, use, transfer, release, disposal, or presence of radioactive material or other

sources of radiation. In part, 10 CFR 20.1201(a) states that the licensee shall control

the occupational dose to individual adults. The licensee violated 10 CFR 20.1501(a)

when it failed to perform an evaluation of airborne radioactivity to ensure compliance

with 10 CFR 20.1201(a). Because this failure to perform a radiological survey was of

very low safety significance and has been entered into the licensees CAP as

CR-RBS-2006-01994, this violation is being treated as an NCV, consistent with

Section VI.A of the NRC Enforcement Policy: NCV 05000458/2006003-05, Failure to

perform airborne radiation survey.

2OS2 ALARA Planning and Controls

a. Inspection Scope

The inspector assessed licensee performance with respect to maintaining individual and

collective radiation exposures ALARA. The inspector used the requirements in 10 CFR

Part 20 and the licensees procedures required by TS as criteria for determining

compliance. The inspector interviewed licensee personnel and reviewed:

  • Current 3-year rolling average collective exposure
  • Three outage or on-line maintenance work activities scheduled during the

inspection period and associated work activity exposure estimates which were

likely to result in the highest personnel collective exposures

  • ALARA work activity evaluations, exposure estimates, and exposure mitigation

requirements

  • Intended versus actual work activity doses and the reasons for any

inconsistencies

  • Shielding requests and dose/benefit analyses
  • Dose rate reduction activities in work planning
  • Use of engineering controls to achieve dose reductions and dose reduction

benefits afforded by shielding

  • Workers use of the low dose waiting areas
  • First-line job supervisors contribution to ensuring work activities are conducted

in a dose efficient manner

-27- Enclosure

  • Radiation worker and radiation protection technician performance during work

activities in radiation areas, airborne radioactivity areas, or high radiation areas

The inspector completed 6 of the required 15 samples and 4 of the optional samples.

b. Findings

No findings of significance were identified.

4. OTHER ACTIVITIES

4OA1 Performance Indicator Verification

a. Inspection Scope

1. Barrier Integrity Cornerstone

The inspectors sampled licensee submittals for the two PIs listed below for the period

October 1, 2004, through March 31, 2006. The definitions and guidance of NEI 99-02,

Regulatory Assessment Indicator Guideline, Revision 4, were used to verify the

licensees basis for reporting each data element in order to verify the accuracy of PI

data reported during the assessment period. The inspectors: (1) reviewed reactor

coolant system (RCS) chemistry sample analyses for dose equivalent Iodine-131 and

compared the results to the TS limit; (2) observed a chemistry technician obtain and

analyze an RCS sample; (3) reviewed operating logs and surveillance results for

measurements of RCS identified leakage; and (4) observed a surveillance test that

determined RCS identified leakage.

C RCS Specific Activity

C RCS Leakage

The inspectors completed two inspection samples.

2. Occupational Radiation Safety Cornerstone

The review included corrective action documentation that identified occurrences in

locked high radiation areas (as defined in the licensees TS), very high radiation areas

(as defined in 10 CFR 20.1003), and unplanned personnel exposures (as defined in

NEI 99-02), specifically CR-RBS-2006-01910. Additional records reviewed included

ALARA records and whole-body counts of selected individual exposures. The inspector

interviewed licensee personnel that were accountable for collecting and evaluating the

PI data. In addition, the inspector toured plant areas to verify that high radiation, locked

high radiation, and very high radiation areas were properly controlled. PI definitions and

guidance contained in NEI 99-02, "Regulatory Assessment Indicator Guideline,"

Revision 3, were used to verify the basis in reporting for each data element.

-28- Enclosure

  • Occupational Exposure Control Effectiveness

The inspector completed the one required sample in this cornerstone.

3. Public Radiation Safety Cornerstone

The inspector reviewed licensee documents from June 1, 2005, through March 31,

2006. Licensee records reviewed included corrective action documentation that

identified occurrences for liquid or gaseous effluent releases that exceeded PI

thresholds and those reported to the NRC. The inspector interviewed licensee

personnel that were accountable for collecting and evaluating the PI data. PI definitions

and guidance contained in NEI 99-02, "Regulatory Assessment Indicator Guideline,"

Revision 3, were used to verify the basis in reporting for each data element.

  • Radiological Effluent Technical Specification/Offsite Dose Calculation Manual

Radiological Effluent Occurrences

The inspector completed the one required sample in this cornerstone.

f. Findings

No findings of significance were identified.

4OA2 Identification and Resolution of Problems

1. Semiannual Trend Review

g. Inspection Scope

The inspectors completed a semiannual trend review of repetitive or closely related

issues related to identify trends that might indicate the existence of more safety

significant issues. The inspectors review consisted of the 6-month period from

January 1 to June 30, 2006, of CAP items associated with the three EDG starting air

systems documented in 42 CRs. When warranted, some of the samples expanded

beyond those dates to fully assess the issue. The inspectors compared and contrasted

their results with the results contained in adverse trend CRs for problems related to the

starting air compressors and air dryers. Corrective actions associated with a sample of

the issues identified were reviewed for adequacy. The CRs reviewed by the inspectors

are listed in the attachment.

The inspectors completed one inspection sample.

b. Findings and Observations

There were no findings of significance identified associated with the CRs reviewed.

The inspectors noted that the licensee had identified a long-standing issue related to the

performance of the EDG starting air systems air compressors. Since January 1, 2006,

-29- Enclosure

there were 18 CRs written for high metal wear products in monthly air compressor oil

samples. Each of these CRs was closed to CR-RBS-2004-02165. An additional

28 CRs written since August 2, 2004, for high metal wear product concentrations and

high moisture content in monthly compressor oil samples were closed to CR-RBS-2004-

02165. In addition, operators wrote adverse trend CR-RBS-2006-02407 to detail

compressor problems, including excessive run times. The inspectors determined that

the licensee is taking appropriate actions to understand the problem with the EDG

starting air compressors, including sending the system engineer to observe the vendors

teardown and refurbishment of two of the starting air compressors.

Another four CRs have been written since January 1, 2006, describing problems with

starting air system dryers and dryer prefilters. Following a June 29, 2006, meeting held

to discuss overall EDG starting air system maintenance problems, the licensee wrote

CR-RBS-2006-02799, to look into the relationship between the prefilter and dryer

problems. The inspectors noted that this meeting was the first discussion of the overall

condition of the EDG starting air systems and to evaluate the interrelationship between

compressor, dryer, and prefilter problems.

2. Occupational Radiation Safety

a. Inspection Scope

The inspector evaluated the effectiveness of the licensees problem identification and

resolution process with respect to the following inspection areas:

  • Access Control to Radiologically Significant Areas (Section 2OS1)
  • ALARA Planning and Controls (Section 2OS2)

b. Findings and Observations

No findings of significance were identified.

3. Inservice Inspection Activities

a. Inspection Scope

The inspector reviewed selected inservice inspection related CRs issued during the

current and past refueling outages. The review served to verify that the licensees CAP

was being correctly utilized to identify conditions adverse to quality and that those

conditions were being adequately evaluated, corrected, and trended.

b. Findings

No findings of significance were identified.

-30- Enclosure

4OA3 Event Followup

1. (Closed) LER 50-458/2004-003-01, Unplanned Automatic Start of Standby Diesel

Generator Due to Loss of Division 1 Switchgear

On October 31, 2004, technicians caused an unexpected degraded voltage signal,

which resulted in a loss of the Division I 4.16 kV ESF bus during preparations for the

Division I loss of offsite power/loss of coolant accident test. The Division I EDG

automatically started and powered the ESF bus and all equipment operated as

expected. Initial inspection of this event was documented in NRC integrated inspection

Report 05000458/2004005. During this inspection period, the inspectors reviewed the

LER, the root cause analysis, and corrective actions documented in

CR-RBS-2004-03518. No additional findings of significance were identified. This LER

is closed.

2. (Closed) LER 50-458/2004-004-01, Unplanned Automatic Start of Standby Diesel

Generator Due to Loss of Division 2 Switchgear

On November 1, 2004, technicians inadvertently caused a trip of Transformer RSS2

preferred station service Transformer RTX-XSR1F while troubleshooting a transformer

sudden pressure relay trip circuit. As a result, power was also lost to preferred station

Transformer RTX-XSR1D and the Division II 4.16 kV ESF bus. The running shutdown

cooling, alternate decay heat removal, and plant operating water cleanup systems lost

power until the Division II EDG started and restored power to the ESF bus. Shutdown

cooling was restored in less than one hour. Initial inspection of this event was

documented in NRC integrated inspection Report 05000458/2004005. During this

inspection period, the inspectors reviewed the LER, the root cause analysis, and

corrective actions documented in CR-RBS-2004-03546. No additional findings of

significance were identified. This LER is closed.

3. (Closed) LER 50-458/2004-005-01, Unplanned Automatic Scram Due to Loss of

Non-Vital 120 Volt Instrument Bus

On December 10, 2004, an automatic scram occurred due to a loss of power to

nonsafety-related instrumentation Bus VBN-PNL01B1. A capacitor on the control board

for the nonsafety-related Inverter BYS-INV01B static switch failed, which caused a loss

of power to Bus VBN-PNL01B1, a subsequent downshift of the plant operating

recirculation pumps and a lockup of the main feedwater regulating valves. The result

was an automatic plant scram complicated by a loss of normal feedwater. Inspection of

this event was documented in NRC integrated inspection Report 05000458/2004005.

Additional inspection was documented in NRC supplemental inspection Report

05000458/2005012. During this inspection period, the inspectors reviewed the LER, the

root cause analysis, and corrective actions documented in CR-RBS-2004-04289. No

additional findings of significance were identified. This LER is closed.

-31- Enclosure

4. (Closed) LER 50-458 /2005-001-01, Unplanned Manual Scram Due to Indication of

Ground Fault in Main Generator

On January 15, 2005, while the plant was at 100 percent power, a main generator field

ground fault alarm was received. Control room operators tripped the turbine in

accordance with alarm response Procedure ARP-680-09. The licensee later determined

that one of the five rectifier banks in the generator excitation control system was the

source of the ground and removed it from service. In addition, the licensee tested the

relay that causes the main generator ground fault alarm and found it to be out of

calibration such that it alarmed before the ground current reached its setpoint. The

alarm response procedure requirement to trip the turbine was revised to allow validation

of the alarm before tripping the main turbine. Inspection of this event was documented

in NRC integrated inspection Report 05000458/2005002. Additional inspection was

documented in NRC supplemental inspection Report 05000458/2005012. During this

inspection period, the inspectors reviewed the LER, the root cause analysis, and

corrective actions documented in CR-RBS-2005-00140. No additional findings of

significance were identified. This LER is closed.

4OA5 Other Activities

Implementation of Temporary Instruction 2515/165 - Operational Readiness of Offsite

Power and Impact on Plant Risk

a. Inspection Scope

The objective of Temporary Instruction 2515/165, "Operational Readiness of Offsite

Power and Impact on Plant Risk," was to gather information to support the assessment

of nuclear power plant operational readiness of offsite power systems and impact on

plant risk. During this inspection, the inspectors interviewed licensee personnel,

reviewed licensee procedures, and gathered information for further evaluation by the

Office of Nuclear Reactor Regulation.

b. Findings

No findings of significance were identified.

4OA6 Meetings, Including Exit

Exit Meetings

On May 5, 2006, the inspector presented the occupational radiation safety inspection

results to Mr. D. Vinci, General Manager, Plant Operations, and other members of his

staff who acknowledged the findings. The inspector confirmed that proprietary

information was not provided or examined during the inspection.

On May 5, 2006, the inspector presented the results of this inspection of inservice

inspection activities to Mr. P. Russell, Manager, System Engineering, and other

-32- Enclosure

members of licensee management. The inspector confirmed that proprietary

information was not provided or examined during the inspection.

On July 5, 2006, the resident inspectors presented the integrated baseline inspection

results to Mr. P. Hinnenkamp, Vice President - Operations, and other members of

licensee management. The inspectors confirmed that proprietary information was not

provided or examined during the inspection.

ATTACHMENT: SUPPLEMENTAL INFORMATION

-33- Enclosure

SUPPLEMENTAL INFORMATION

KEY POINTS OF CONTACT

Licensee Personnel

T. Baccus, Acting Supervisor, ALARA Planning

L. Ballard, Manager, Quality Programs

D. Burnett, Superintendent, Chemistry

C. Bush, Manager, Outage

J. Clark, Assistant Operations Manager - Training

T. Coleman, Manager, Planning and Scheduling/Outage

M. Davis, Manager, Radiation Protection

C. Forpahl, Manager, Corrective Action Program

T. Gates, Manager, Equipment Reliability

H. Goodman, Director, Engineering

K. Higginbotham, Assistant Operations Manager - Shift

P. Hinnenkamp, Vice President - Operations

B. Houston, Manager, Plant Maintenance

A. James, Superintendent, Plant Security

K. Jenks, Supervisor, Engineering Codes and Standards

N. Johnson, Manager, Engineering Programs & Components

R. King, Director, Nuclear Safety Assurance

J. Leavines, Manager, Emergency Planning

D. Lorfing, Manager, Licensing

J. Maher, Superintendent, Reactor Engineering

W. Mashburn, Manager, Design Engineering

J. Miller, Manager, Training and Development

P. Russell, Manager, System Engineering

C. Stafford, Manager, Operations

D. Vinci, General Manager - Plant Operations

LIST OF ITEMS OPENED, CLOSED, AND DISCUSSED

Opened and Closed

05000458/2006003-01 NCV Failure to identify Division III ESF bus supply breaker not

racked in

05000458/2006003-02 NCV Failure to adequately manage an increase in plant risk

05000458/2006003-03 NCV Inadequate procedure to verify required offsite power

breaker alignment

05000458/2006003-04 NCV Failure to control access to a high radiation area

05000458/2006003-05 NCV Failure to perform airborne radiation survey

A-1 Attachment

Closed

50-458/2004-003-01 LER Unplanned Automatic Start of Standby Diesel Generator

Due to Loss of Division 1 Switchgear

50-458/2004-004-01 LER Unplanned Automatic Start of Standby Diesel Generator

Due to Loss of Division 2 Switchgear

50-458/2004-005-01 LER Unplanned Automatic Scram Due to Loss of Non-Vital 120

Volt Instrument Bus

50-458 /2005-001-01 LER Unplanned Manual Scram Due to Indication of Ground

Fault in Main Generator

LIST OF DOCUMENTS REVIEWED

The following documents were selected and reviewed by the inspectors to accomplish the

objectives and scope of the inspection and to support any findings:

Section 1R06: Inservice Inspection Activities

Procedures

CEP-NDE-0400, Ultrasonic Examination, Revision 0

CEP-NDE-0404, Manual Ultrasonic Examination of Ferritic Piping Welds (ASME XI),

Revision 1

CEP-NDE-0407, Straight Beam Ultrasonic Examination of Bolts and Studs (ASME XI),

Revision 1

CEP-NDE-0423, Manual Ultrasonic Examination of Austenitic Piping Welds (ASME XI),

Revision 1

CEP-NDE-0424, Manual Ultrasonic Examination of the Reactor Vessel Flange Ligament Areas

(ASME XI), Revision 1

CEP-NDE-0428, Manual Ultrasonic Throughwall Sizing in Piping Welds (ASME XI), Revision 1

CEP-NDE-0641, Liquid Penetrant Examination for ASME Section XI, Revision 1

CEP-NDE-0731, Magnetic Particle Examination (ASME Section XI), Revision 0

SPP-7010, Preparation of Weld Data Documents, Revision 9

A-2 Attachment

Miscellaneous Documents

7228.000-701-131A, Risk Informed Break Exclusion Region Evaluation for River Bend

Station, Revision 0

Liquid Penetrant Examinations

BOP-PT-06-024 BOP-PT-06-025 BOP-PT-06-026 BOP-PT-06-029

UT Calibration Reports

CAL -06-015 CAL -06-016 CAL-06-017

UT Pipe Weld Examinations

ISI-UT-06-003 ISI-UT-06-006 ISI-UT-06-009 ISI-UT-06-012

ISI-UT-06-004 ISI-UT-06-007 ISI-UT-06-010 ISI-UT-06-013

ISI-UT-06-005 ISI-UT-06-008 ISI-UT-06-011 ISI-UT-06-014

Condition Reports

CR-RBS-2005-00065 CR-RBS-2005-00067 CR-RBS-2005-00100 CR-RBS-2005-01379

Section 1R15: Operability Evaluations

Primary Containment Purge Exhaust Line Operability

CR-RBS-2006-00964, primary containment purge exhaust line leak rate test results showing

negative trend

ADM-0050, Primary Containment Leakage Rate Testing Program, Revision 8

SEP-APJ-001, Primary containment Leakage Rate Testing (Appendix J) Program,

Revision 0G

STP-403-7301, Containment Purge System Isolation Valve Leak Rate Test, Revisions 0, 1, 2,

and 3

RBS-ER-00-0589, Post RF-09 LLRT Testing Interval Determination, dated January 25, 2001

RBS TS Amendment 81, dated July 20, 1995

RBS TS Bases Revision 126, dated March 31, 206

Attachment

NNS-ACB23 Not Functional

Electrical Drawings

EE-001AC, Startup Electrical Distribution Chart, Revision 33

ESK-05NNS03, Elementary Diagram - 4.16 kV Switchgear Bus 1C Normal Supply ACB,

Revision 13

Corrective Action Documents

CR-RBS-2006-02402 CR-RBS-2006-0235 CR-RBS-2006-02337

CR-RBS-1998-00190

Procedures

OSP-0022, Operations General Administrative Guidelines, Revision 01

GOP-0001, Plant Startup, Revision 47, performed on May 12, 2006

STP-000-0102, Power Distribution Alignment Check, Revision 4, performed on May 9, 2006

STP-000-0102, Power Distribution Alignment Check, Revision 4, performed on May 22, 2006

Work Requests

WR 76625 WR 77441 WR77478

Miscellaneous Documents

Main Control Room Logs

TS LCO Records: 1-OPT-06-0187 1-TS-06-0694

RBS Tagout Record: 1-302-NNS-SWG1A-006-A

Section 1R20: Refueling and Other Outage Activities

Procedures

RSP-0217, Auxiliary Access Control Functions, Revision 27

GOP-0003, Scram Recovery, Revision 14A, post scram report, dated April 23, 2006

OSP-0031, Shutdown Operations Protection Plan, Revision 16

OSP-0041, Alternate Decay Heat Removal, Revision 8A

AOP-0051, Loss of Decay Heat Removal, Revision 18

OSP-0034, Control of Obstructions for Primary Containment/Fuel Building Operability,

Revision 3

A-4 Attachment

GOP-0001, Plant Startup, Revision 47, performed on May 12, 2006

Corrective Action Documents

CR-RBS-2006-00691 CR-RBS-2006-01937

Miscellaneous Documents

Control Room Logs

TS LCO Logs

Daily Refueling Outage Updates

ORAT Report

WO 50340401 and 81284

ER-RB-2005-0157-000, Install new relays on the output of EOC-RPT optical output cards

C71A-AT17 and C71A-AT18, dated May 16, 2006

WO 5034041's task outline to configure the station blackout diesel to supply power to spent fuel

pool cooling Pump SFC-P1A

WO 5034041, Configure the station blackout diesel to supply power to spent fuel pool cooling

Pump SFC-P1A, written May 3, 2006

Section 1R22: Surveillance Testing

Drawing EE-001AC, Startup Electrical Distribution Chart, Revision 33

TS Section 3.8.1 and Bases 3.8.1, Revision 0

USAR Section 8.2.1.2.1, General Design Criteria, Revision 16

NUREG-0989, Safety Evaluation Report Related to the Operation of River Bend Station,

dated May 1984

TS LCO Logs

1-TS-06-0694 I-TS-06-0685 1-TS-05-0386

Corrective Action Documents

CR-RBS-2006-02675 CR-RBS-2006-02402 CR-RBS-2005-02331

A-5 Attachment

Section 4OA2: Identification and Resolution of Problems

Semiannual Trend Review

CR-RBS-2004-02165 CR-RBS-2006-01270 CR-RBS-2006-02469

CR-RBS-2006-00159 CR-RBS-2006-01324 CR-RBS-2006-02484

CR-RBS-2006-00226 CR-RBS-2006-01333 CR-RBS-2006-02540

CR-RBS-2006-00279 CR-RBS-2006-01429 CR-RBS-2006-02544

CR-RBS-2006-00296 CR-RBS-2006-01464 CR-RBS-2006-02550

CR-RBS-2006-00434 CR-RBS-2006-01489 CR-RBS-2006-02558

CR-RBS-2006-00663 CR-RBS-2006-01490 CR-RBS-2006-02559

CR-RBS-2006-00798 CR-RBS-2006-02269 CR-RBS-2006-02651

CR-RBS-2006-00799 CR-RBS-2006-02348 CR-RBS-2006-02661

CR-RBS-2006-00928 CR-RBS-2006-02349 CR-RBS-2006-02682

CR-RBS-2006-00993 CR-RBS-2006-02356 CR-RBS-2006-02683

CR-RBS-2006-01131 CR-RBS-2006-02375 CR-RBS-2006-02732

CR-RBS-2006-01132 CR-RBS-2006-02406 CR-RBS-2006-02733

CR-RBS-2006-01205 CR-RBS-2006-02407 CR-RBS-2006-02799

CR-RBS-2006-01261

Section 2OS1: Access Controls to Radiologically Significant Areas

Corrective Action Documents

CR-RBS-2006-00090 CR-RBS- 2006-01294 CR-RBS-2006-01787 CR-RBS- 2006-01950

Radiation Work Permits

2006-1915 RFO-13, Remove and Replace LPRMs, Including Support Activities

2006-1921 RFO-13, Flow Control Valve Maintenance, Including Support Activities

2006-1929 RFO-13, Recirc Pump Work, Including Support Activities

Procedures

RP-103 Access Control, Revision 2

RP-106 Radiological Survey Documentation, Revision 1

RP-108 Radiation Protection Posting, Revision 2

RPP-0006 Performance of Radiological Surveys, Revision 19

Section 2OS2: ALARA Planning and Controls (71121.02)

Corrective Action Documents

CR-RBS-2006-01746

Procedures

ENS-RP-105 Radiation Work Permits, Revision 7

A-6 Attachment

LIST OF ACRONYMS

CDF core damage frequency

ALARA as low as is reasonably achievable

ASME American Society of Mechanical Engineers

CAP corrective action program

CFR Code of Federal Regulations

CR-RBS River Bend Station condition report

EDG emergency diesel generator

LER licensee event report

MC inspection manual chapter

NCV noncited violation

NDE nondestructive examination

NEI Nuclear Energy Institute

NRC U.S. Nuclear Regulatory Commission

ORAT outage risk assessment team

PI performance indicators

RCS reactor coolant system

RFO refueling outage

SFC spent fuel pool cooling system

SOP system operating procedures

SR surveillance requirement

SSC structures, systems, or components

STP surveillance test procedure

TS Technical Specifications

USAR Updated Safety Analysis Report

WO work order

WR work request

A-7 Attachment