ML070300881: Difference between revisions

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{{#Wiki_filter:January 30, 2007Tennessee Valley AuthorityATTN:Mr. Karl W. SingerChief Nuclear Officer and
{{#Wiki_filter:January 30, 2007
  Executive Vice President6A Lookout Place
Tennessee Valley Authority
ATTN: Mr. Karl W. Singer
        Chief Nuclear Officer and
          Executive Vice President
6A Lookout Place
1101 Market Street
1101 Market Street
Chattanooga, TN 37402-2801SUBJECT:SEQUOYAH NUCLEAR PLANT - NRC INTEGRATED INSPECTION REPORT05000327/2006005, 05000328/2006005 AND 07200034/2006002Dear Mr. Singer:
Chattanooga, TN 37402-2801
On December 31, 2006, the United States Nuclear Regulatory Commission (NRC) completedan inspection at your Sequoyah Nuclear Plant, Units 1 and 2. The enclosed integrated
SUBJECT:       SEQUOYAH NUCLEAR PLANT - NRC INTEGRATED INSPECTION REPORT
                05000327/2006005, 05000328/2006005 AND 07200034/2006002
Dear Mr. Singer:
On December 31, 2006, the United States Nuclear Regulatory Commission (NRC) completed
an inspection at your Sequoyah Nuclear Plant, Units 1 and 2. The enclosed integrated
inspection report documents the inspection results, which were discussed on January 3, 2007,
inspection report documents the inspection results, which were discussed on January 3, 2007,
with Mr. R. Duet and other members of your staff.The inspection examined activities conducted under your licenses as they relate to safety andcompliance with the Commission's rules and regulations and with the conditions of your
with Mr. R. Duet and other members of your staff.
licenses. The inspectors reviewed selected procedures and records, observed activities, and
The inspection examined activities conducted under your licenses as they relate to safety and
interviewed personnel.The report documents one NRC-identified finding of very low safety significance. This findingwas determined to involve a violation of NRC requirements. Additionally, a licensee-identified
compliance with the Commissions rules and regulations and with the conditions of your
violation which was determined to be of very low safety significance is listed in this report.  
licenses. The inspectors reviewed selected procedures and records, observed activities, and
interviewed personnel.
The report documents one NRC-identified finding of very low safety significance. This finding
was determined to involve a violation of NRC requirements. Additionally, a licensee-identified
violation which was determined to be of very low safety significance is listed in this report.
However, because of their very low safety significance and because they are entered into your
However, because of their very low safety significance and because they are entered into your
corrective action program, the NRC is treating these findings as non-cited violations (NCVs)
corrective action program, the NRC is treating these findings as non-cited violations (NCVs)
consistent with Section VI.A.1 of the NRC Enforcement Policy. If you contest any NCV in this
consistent with Section VI.A.1 of the NRC Enforcement Policy. If you contest any NCV in this
report, you should provide a response within 30 days of the date of this inspection report, with
report, you should provide a response within 30 days of the date of this inspection report, with
the basis for your denial, to the United States Nuclear Regulatory Commission, ATTN.:
the basis for your denial, to the United States Nuclear Regulatory Commission, ATTN.:
Line 35: Line 47:
Administrator Region II; the Director, Office of Enforcement, United States Nuclear Regulatory
Administrator Region II; the Director, Office of Enforcement, United States Nuclear Regulatory
Commission, Washington, D.C. 20555-0001; and the NRC Resident Inspector at the Sequoyah
Commission, Washington, D.C. 20555-0001; and the NRC Resident Inspector at the Sequoyah
Nuclear Plant.In accordance with 10 CFR 2.390 of the NRC's "Rules of Practice," a copy of this letter, itsenclosure, and your response (if any) will be available electronically for public inspection in the
Nuclear Plant.
NRC Public Document Room or from the Publically Available Records (PARS) component of
In accordance with 10 CFR 2.390 of the NRC's "Rules of Practice," a copy of this letter, its
2NRC's document system (ADAMS). ADAMS is accessible from the NRC Website athttp://www.nrc.gov/reading-rm/adams.html
enclosure, and your response (if any) will be available electronically for public inspection in the
(the Public Electronic Reading Room).Sincerely,/RA/Malcolm T. Widmann, ChiefReactor Projects Branch 6
NRC Public Document Room or from the Publically Available Records (PARS) component of
Division of Reactor ProjectsDocket Nos.:50-327, 50-328, 72-034License Nos.:DPR-77, DPR-79Enclosure: Inspection Report 05000327/2006005 and 05000328/2006005 and07200034/2006002 w/Attachment: Supplemental Informationcc: w/encl: (See page 3)  
 
                                              2
NRCs document system (ADAMS). ADAMS is accessible from the NRC Website at
http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room).
                                          Sincerely,
                                          /RA/
                                          Malcolm T. Widmann, Chief
                                          Reactor Projects Branch 6
                                          Division of Reactor Projects
Docket Nos.: 50-327, 50-328, 72-034
License Nos.: DPR-77, DPR-79
Enclosure: Inspection Report 05000327/2006005 and 05000328/2006005 and
              07200034/2006002 w/Attachment: Supplemental Information
cc: w/encl: (See page 3)
 


____ML070300881   
____ML070300881 __
__OFFICERII:DRPRII:DRPRII:DRPRII:DRPRII:DRSRII:DRSRII:DRSSIGNATURELXG /RA/WTM /RA/JBB via emailMES via emailJXD /RA/FJE /RA/LFL /RA/NAMELGarnerMWidmannJBaptistMSpeckJDiaz-VelezFEhrhardtLLakeDATE01/30/200701/30/200701/30/200701/30/200701/30/200701/30/200701/30/2007
  OFFICE            RII:DRP        RII:DRP      RII:DRP          RII:DRP        RII:DRS      RII:DRS      RII:DRS
E-MAIL COPY?   YESNO     YESNO      YESNO      YESNO      YESNO      YESNO      YESNO   OFFICERII:DRSRII:DRSRII:DRSRII:DRSRII:DRSRII:DRSRII:DRSSIGNATUREGWL /RA/DLM /RA/ECM /RA/BWM /RA/CRO forSDR /RA/CRO forNAMEGLaskaDMasPenarandaEMichelBMillerRMooreSRoseCSmithDATE01/30/200701/30/200701/30/200701/30/200701/30/200701/30/200701/30/2007
SIGNATURE          LXG /RA/       WTM /RA/     JBB via email    MES via email  JXD /RA/     FJE /RA/     LFL /RA/
E-MAIL COPY?   YESNO     YESNO      YESNO      YESNO      YESNO      YESNO      YESNO   OFFICERII:DRSSIGNATURECRS /RA/NAMECStancilDATE01/30/2007
NAME              LGarner        MWidmann      JBaptist        MSpeck          JDiaz-Velez  FEhrhardt    LLake
E-MAIL COPY?   YESNO     YESNO      YESNO      YESNO      YESNO      YESNO      YESNO      
DATE                  01/30/2007    01/30/2007    01/30/2007      01/30/2007      01/30/2007    01/30/2007    01/30/2007
3cc w/encls:Ashok S. Bhatnagar
E-MAIL COPY?         YES     NO  YES      NO  YES      NO    YES      NO   YES      NO  YES      NO  YES      NO
OFFICE            RII:DRS        RII:DRS      RII:DRS          RII:DRS        RII:DRS      RII:DRS      RII:DRS
SIGNATURE          GWL /RA/       DLM /RA/     ECM /RA/         BWM /RA/       CRO for      SDR /RA/     CRO for
NAME              GLaska        DMasPenaranda EMichel          BMiller        RMoore        SRose        CSmith
DATE                  01/30/2007    01/30/2007    01/30/2007      01/30/2007      01/30/2007    01/30/2007    01/30/2007
E-MAIL COPY?         YES     NO  YES      NO  YES      NO    YES      NO   YES      NO  YES      NO  YES      NO
OFFICE            RII:DRS
SIGNATURE          CRS /RA/
NAME              CStancil
DATE                  01/30/2007
E-MAIL COPY?         YES     NO  YES      NO  YES      NO     YES      NO    YES      NO  YES      NO  YES      NO
       
                                  3
cc w/encls:
Ashok S. Bhatnagar                   Beth A. Wetzel, Manager
Senior Vice President                Corporate Nuclear Licensing and
Nuclear Operations                    Industry Affairs
Tennessee Valley Authority          Tennessee Valley Authority
Electronic Mail Distribution        4X Blue Ridge
                                    1101 Market Street
Preston D. Swafford                  Chattanooga, TN 37402-2801
Senior Vice President
Senior Vice President
Nuclear Operations
Nuclear Support                      Robert H. Bryan, Jr., General Manager
Tennessee Valley Authority
Tennessee Valley Authority           Licensing and Industry Affairs
Electronic Mail DistributionPreston D. SwaffordSenior Vice President
Electronic Mail Distribution        Sequoyah Nuclear Plant
Nuclear Support
                                    Tennessee Valley Authority
Tennessee Valley Authority
Larry S. Bryant, Vice President      4X Blue Ridge
Electronic Mail DistributionLarry S. Bryant, Vice PresidentNuclear Engineering &
Nuclear Engineering &               1101 Market Street
Technical Services
Technical Services                   Chattanooga, TN 37402-2801
Tennessee Valley Authority
Tennessee Valley Authority
Electronic Mail DistributionRandy DouetSite Vice President
Electronic Mail Distribution        David A. Kulisek, Plant Manager
                                    Sequoyah Nuclear Plant
Randy Douet                          Tennessee Valley Authority
Site Vice President                 Electronic Mail Distribution
Sequoyah Nuclear Plant
Sequoyah Nuclear Plant
Electronic Mail DistributionGeneral CounselTennessee Valley Authority
Electronic Mail Distribution        Lawrence E. Nanney, Director
Electronic Mail DistributionJohn C. Fornicola, General ManagerNuclear Assurance  
                                    TN Dept. of Environment & Conservation
General Counsel                      Division of Radiological Health
Tennessee Valley Authority           Electronic Mail Distribution
Electronic Mail Distribution
                                    County Mayor
John C. Fornicola, General Manager  Hamilton County Courthouse
Nuclear Assurance                   Chattanooga, TN 37402-2801
Tennessee Valley Authority
Tennessee Valley Authority
Electronic Mail DistributionGlenn W. Morris, ManagerLicensing and Industry Affairs
Electronic Mail Distribution        Ann Harris
Sequoyah Nuclear Plant
                                    341 Swing Loop
Tennessee Valley Authority
Glenn W. Morris, Manager            Rockwood, TN 37854
Electronic Mail DistributionBeth A. Wetzel, ManagerCorporate Nuclear Licensing and
Licensing and Industry Affairs
  Industry Affairs
Sequoyah Nuclear Plant               James H. Bassham, Director
Tennessee Valley Authority
Tennessee Valley Authority           Tennessee Emergency Management
4X Blue Ridge
Electronic Mail Distribution        Agency
1101 Market Street
                                    Electronic Mail Distribution
Chattanooga, TN 37402-2801Robert H. Bryan, Jr., General  ManagerLicensing and Industry Affairs
                                    Distribution w/encl: (See page 4)
Sequoyah Nuclear Plant
 
Tennessee Valley Authority
                                            4
4X Blue Ridge
Letter to Karl W. Singer from Malcolm T. Widmann dated January 30, 2007
1101 Market Street
SUBJECT:       SEQUOYAH NUCLEAR PLANT - NRC INTEGRATED INSPECTION REPORT
Chattanooga, TN 37402-2801David A. Kulisek, Plant ManagerSequoyah Nuclear Plant
                05000327/2006005, 05000328/2006005 AND 07200034/2006002
Tennessee Valley Authority
Distribution w/encl:
Electronic Mail DistributionLawrence E. Nanney, DirectorTN Dept. of Environment & Conservation
Bob Pascarelli, NRR
Division of Radiological Health
Electronic Mail DistributionCounty MayorHamilton County Courthouse
Chattanooga, TN  37402-2801Ann Harris341 Swing Loop
Rockwood, TN  37854
James H. Bassham, DirectorTennessee Emergency Management
Agency
Electronic Mail DistributionDistribution w/encl: (See page 4)  
4Letter to Karl W. Singer from Malcolm T. Widmann dated January 30, 2007SUBJECT:SEQUOYAH NUCLEAR PLANT - NRC INTEGRATED INSPECTION REPORT05000327/2006005, 05000328/2006005 AND 07200034/2006002Distribution w/encl
:Bob Pascarelli, NRR
D. Pickett, NRR
D. Pickett, NRR
C. Evans, RII
C. Evans, RII
Line 91: Line 137:
OE Mail
OE Mail
RIDSNRRDIRS
RIDSNRRDIRS
PUBLIC  
PUBLIC
TABLE OF CONTENTSSUMMARY OF FINDINGS....................................................2REPORT DETAILS..........................................................3
 
REACTOR SAFETY.........................................................31R01Adverse Weather Protection.......................................41R02Evaluations of Changes, Tests or Experiments.........................41R04Equipment Alignment.............................................41R05Fire Protection..................................................41R07Heat Sink Performance...........................................51R08Inservice Inspection (ISI) Activities...................................61R11Licensed Operator Requalification Program............................91R12Maintenance Effectiveness.......................................121R13Maintenance Risk Assessments and Emergent Work Control.............121R15Operability Evaluations..........................................131R17Permanent Plant Modifications.....................................151R19Post-Maintenance Testing........................................161R20Refueling and Other Outage Activities...............................171R22Surveillance Testing.............................................191EP6Drill Evaluation.................................................19RADIATION SAFETY.......................................................202OS1Access Control To Radiologically Significant Areas.....................20OTHER ACTIVITIES........................................................214OA2Identification & Resolution of Problems..............................214OA5Other Activities.................................................234OA6Management Meetings...........................................294OA7  Licensee Identified Violations......................................29ATTACHMENT: SUPPLEMENTARY INFORMATIONKey Points of Contact......................................................A-1
                                            TABLE OF CONTENTS
List of Items Opened, Closed, and Discussed....................................A-1List of Documents Reviewed.................................................A-3
SUMMARY OF FINDINGS . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 2
List of Acronyms.........................................................A-14  
REPORT DETAILS . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 3
EnclosureU. S. NUCLEAR REGULATORY COMMISSIONREGION IIDocket Nos:50-327, 50-328, 72-034License Nos:DPR-77, DPR-79
REACTOR SAFETY . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 3
Report No:05000327/2006005 and 05000328/2006005 and07200034/2006002Licensee:Tennessee Valley Authority (TVA)
        1R01 Adverse Weather Protection . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 4
Facility:Sequoyah Nuclear Plant
        1R02 Evaluations of Changes, Tests or Experiments . . . . . . . . . . . . . . . . . . . . . . . . . 4
Location:Sequoyah Access RoadSoddy-Daisy, TN 37379Dates:October 1, 2006 - December 31, 2006
        1R04 Equipment Alignment . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 4
Inspectors:J. Baptist, Acting Senior Resident InspectorJ. Diaz-Velez, Health Physicist (Section 2OS1)
        1R05 Fire Protection . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 4
F. Ehrhardt, Operations Engineer (Section 1R11.2)
        1R07 Heat Sink Performance . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 5
L. Lake, Reactor Inspector (Section 1R08)
        1R08 Inservice Inspection (ISI) Activities . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 6
G. Laska, Senior Operations Examiner (Section 1R11.3)  
        1R11 Licensed Operator Requalification Program . . . . . . . . . . . . . . . . . . . . . . . . . . . . 9
D. Mas-Penaranda, Reactor Inspector (Sections 1R02, 1R17)
        1R12 Maintenance Effectiveness . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 12
E. Michel, Reactor Inspector (Section 4OA5.3)
        1R13 Maintenance Risk Assessments and Emergent Work Control . . . . . . . . . . . . . 12
B. Miller, Reactor Inspector (Sections 1R08, 4OA5.2)
        1R15 Operability Evaluations . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 13
R. Moore, Senior Reactor Inspector (Section 4OA5.3)
        1R17 Permanent Plant Modifications . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 15
S. Rose, Senior Operations Engineer (Section 1R11.3)
        1R19 Post-Maintenance Testing . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 16
C. Smith Senior Reactor Inspector (Sections 1R02, 1R17)
        1R20 Refueling and Other Outage Activities . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 17
M. Speck, Resident Inspector
        1R22 Surveillance Testing . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 19
C. Stancil, Resident Inspector (Section 1EP6)Approved by:M. Widmann, Chief Reactor Projects Branch 6
        1EP6 Drill Evaluation . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 19
Division of Reactor Projects  
RADIATION SAFETY . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 20
EnclosureSUMMARY OF FINDINGSIR 05000327/2006005, IR 05000328/2006005; IR 07200034/2006002; 10/01/2006 -12/31/2006; Sequoyah Nuclear Plant, Units 1 & 2; Licensed Operator Requalification
        2OS1 Access Control To Radiologically Significant Areas . . . . . . . . . . . . . . . . . . . . . 20
Program.The report covered a three-month period of inspection by resident inspectors andannounced inspections by 10 regional inspectors and one resident inspector from
OTHER ACTIVITIES . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . .     21
another site. One NRC-identified Green finding, which was also a non-cited violation,
        4OA2 Identification & Resolution of Problems . . . . . . . . . . . . . . . . . . . . . . . . . . . . . .                   21
was identified. The significance of most findings is indicated by their color (Green,
        4OA5 Other Activities . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . .     23
White, Yellow, Red) using Inspection Manual Chapter (IMC) 0609, "Significance
        4OA6 Management Meetings . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . .             29
Determination Process" (SDP). Findings for which the SDP does not apply may be
        4OA7 Licensee Identified Violations . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . .             29
Green or be assigned a severity level after NRC management review. The NRC's
ATTACHMENT: SUPPLEMENTARY INFORMATION
program for overseeing the safe operation of commercial nuclear power reactors is
Key Points of Contact . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . A-1
described in NUREG-1649, "Reactor Oversight Process," Revision 3, dated July 2000.A.NRC-Identified and Self-Revealing FindingsCornerstone:Mitigating Systems
List of Items Opened, Closed, and Discussed . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . A-1
Green. The inspectors identified a Green, non-cited violation (NCV) of 10 CFR 55.53,"Conditions of Licenses" for failure to certify the qualifications and status of licensed
List of Documents Reviewed . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . A-3
operators were current and valid prior to their resumption of license duties. Specific
List of Acronyms . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . A-14
aspects of the requalification program that were not valid included plant tours that were
 
not completed with another licensed operator and not completing all shift functions in  
            U. S. NUCLEAR REGULATORY COMMISSION
positions to which the individuals will be assigned. The licensee entered the finding into
                                REGION II
the corrective action program as PER No.112004. The finding is greater than minor because it is associated with the human performanceattribute of the Mitigating Systems Cornerstone that affects the cornerstone objective of
Docket Nos:       50-327, 50-328, 72-034
ensuring the availability, reliability, and capability of operators to respond to initiating
License Nos:       DPR-77, DPR-79
events to prevent undesirable consequences that could pose a potential risk to
Report No:         05000327/2006005 and 05000328/2006005 and
operations. The finding was evaluated using the Operator Requalification Human
                  07200034/2006002
Performance Significance Determination Process. Under this SDP, record deficienciescan be either minor or of very low safety significance (Green). This finding was
Licensee:         Tennessee Valley Authority (TVA)
determined to be Green because it was related to the program for maintaining active
Facility:         Sequoyah Nuclear Plant
licenses and more than 20% of the records reviewed had deficiencies. (Section 1R11.3).B. Licensee-Identified ViolationsA violation of very low safety significance, which was identified by the licensee, wasreviewed by the inspectors. Corrective actions taken or planned by the licensee have
Location:         Sequoyah Access Road
been entered into the licensee's corrective action program. This violation and corrective
                  Soddy-Daisy, TN 37379
action are listed in Section 4OA7.  
Dates:             October 1, 2006 - December 31, 2006
EnclosureREPORT DETAILSSummary of Plant Status
Inspectors:       J. Baptist, Acting Senior Resident Inspector
:Unit 1 operated at or near 100% rated thermal power (RTP) for the duration of thereporting period.Unit 2 operated at or near 100% RTP until November 27, 2006 when it shut down for arefueling outage. Unit 2 achieved criticality on December 24, 2006, and reached 100%
                  J. Diaz-Velez, Health Physicist (Section 2OS1)
RTP on December 29, 2006, where it remained for the duration of the reporting period.1.REACTOR SAFETYCornerstones: Initiating Events, Mitigating Systems, and Barrier Integrity1R01Adverse Weather Protection    a.Inspection ScopeThe inspectors reviewed design features and licensee preparations for protecting theessential raw cooling water (ERCW) intake structure and both Unit 1 and 2 refueling
                  F. Ehrhardt, Operations Engineer (Section 1R11.2)
water storage tanks (RWSTs) from extreme cold and freezing conditions. The
                  L. Lake, Reactor Inspector (Section 1R08)
inspectors reviewed the Updated Final Safety Analysis Report (UFSAR), and Technical
                  G. Laska, Senior Operations Examiner (Section 1R11.3)
Specifications (TS), reviewed and observed implementation of licensee freeze protection
                  D. Mas-Penaranda, Reactor Inspector (Sections 1R02, 1R17)
procedures, and walked down portions of the systems to assess the status of system
                  E. Michel, Reactor Inspector (Section 4OA5.3)
deficiencies and the system readiness for extreme cold weather. Inspectors performed
                  B. Miller, Reactor Inspector (Sections 1R08, 4OA5.2)
corrective action program keyword searches to verify deficiencies were being identified
                  R. Moore, Senior Reactor Inspector (Section 4OA5.3)
at an appropriate level and that actions were taken to correct problems. Documents
                  S. Rose, Senior Operations Engineer (Section 1R11.3)
reviewed are listed in the Attachment to this report.    b.FindingsNo findings of significance were identified.1R02Evaluations of Changes, Tests or Experiments    a.Inspection Scope
                  C. Smith Senior Reactor Inspector (Sections 1R02, 1R17)
The inspectors reviewed selected samples of 10 CFR 50.59 evaluations to verify that
                  M. Speck, Resident Inspector
the licensee had appropriately considered the conditions under which changes to the
                  C. Stancil, Resident Inspector (Section 1EP6)
facility, Updated Final Safety Analysis Report (UFSAR), or procedures may be made,
Approved by:       M. Widmann, Chief
and tests conducted, without prior NRC approval. The inspectors reviewed ten
                  Reactor Projects Branch 6
evaluations completed for changes made by the licensee without prior NRC approval.  
                  Division of Reactor Projects
The inspectors also reviewed documents prepared in connection with the changes.
                                                                        Enclosure
Documents reviewed included supporting analyses, the UFSAR, and drawings to verify
 
that the licensee had correctly concluded that the changes could be made without
                                SUMMARY OF FINDINGS
obtaining a license amendment. The ten evaluations reviewed are listed in the
  IR 05000327/2006005, IR 05000328/2006005; IR 07200034/2006002; 10/01/2006 -
Attachment to this report.  
  12/31/2006; Sequoyah Nuclear Plant, Units 1 & 2; Licensed Operator Requalification
4EnclosureAdditionally, the inspectors reviewed samples of changes for which the licensee haddetermined that evaluations were not required. The reviews were performed to verify
  Program.
that the licensee's conclusions to "screen out" these changes were correct, and the
  The report covered a three-month period of inspection by resident inspectors and
changes were made in compliance with the requirements of 10 CFR 50.59. The sixteen  
  announced inspections by 10 regional inspectors and one resident inspector from
"screened out" changes reviewed are listed in the Attachment to this report.The inspectors also reviewed selected problem evaluation reports (PERs) to verify thatplant problems were evaluated for root/apparent causes; extent of condition; and that
  another site. One NRC-identified Green finding, which was also a non-cited violation,
the developed corrective actions were adequate to ensure recurrence control of the
  was identified. The significance of most findings is indicated by their color (Green,
identified plant problem.     b.FindingsNo findings of significance were identified.1R04Equipment Alignment   a.Inspection ScopePartial System Walkdowns. The inspectors performed a partial walkdown of thefollowing three systems to verify the operability of redundant or diverse trains and
  White, Yellow, Red) using Inspection Manual Chapter (IMC) 0609, "Significance
components when safety equipment was inoperable. The inspectors attempted to
  Determination Process" (SDP). Findings for which the SDP does not apply may be
identify any discrepancies that could impact the function of the system, and, therefore,
  Green or be assigned a severity level after NRC management review. The NRC's
potentially increase risk. The inspectors reviewed applicable operating procedures,
  program for overseeing the safe operation of commercial nuclear power reactors is
walked down control system components and verified that selected breakers, valves,
  described in NUREG-1649, "Reactor Oversight Process," Revision 3, dated July 2000.
and support equipment were in the correct position to support system operation. The
A. NRC-Identified and Self-Revealing Findings
inspectors also verified that the licensee had properly identified and resolved equipment
  Cornerstone: Mitigating Systems
alignment problems that could cause initiating events or impact the capability of
  Green. The inspectors identified a Green, non-cited violation (NCV) of 10 CFR 55.53,
mitigating systems or barriers and entered them into the corrective action program.  
  Conditions of Licenses for failure to certify the qualifications and status of licensed
Documents reviewed are listed in the Attachment to this report.*Residual Heat Removal (RHR) Train 2B during maintenance on Train 2A*Emergency Diesels 1A, 1B, and 2A during diesel 2B Outage
  operators were current and valid prior to their resumption of license duties. Specific
*Unit 2 Spent Fuel Pool Cooling during full core offload   b.FindingsNo findings of significance were identified.1R05Fire Protection   a.Inspection ScopeThe inspectors conducted a tour of the eight areas listed below to assess the material
  aspects of the requalification program that were not valid included plant tours that were
condition and operational status of fire protection features. The inspectors verified that
  not completed with another licensed operator and not completing all shift functions in
combustibles and ignition sources were controlled in accordance with the licensee's
  positions to which the individuals will be assigned. The licensee entered the finding into
administrative procedures, fire detection and suppression equipment was available for
  the corrective action program as PER No.112004.
use; that passive fire barriers were maintained in good material condition; and that
  The finding is greater than minor because it is associated with the human performance
compensatory measures for out-of-service, degraded, or inoperable fire protection  
  attribute of the Mitigating Systems Cornerstone that affects the cornerstone objective of
5Enclosureequipment were implemented in accordance with the licensee's fire plan. Documentsreviewed are listed in the Attachment to this report.*Control Building Elevation 669 (Mechanical Equipment Room, 250-VDC Batteryand Battery Board Rooms)*Control Building Elevation 706 (Cable Spreading Room)
  ensuring the availability, reliability, and capability of operators to respond to initiating
*Control Building Elevation 685 (Auxiliary Instrument Rooms)
  events to prevent undesirable consequences that could pose a potential risk to
*Auxiliary Building Elevation 690 (Corridor)
  operations. The finding was evaluated using the Operator Requalification Human
*Emergency Diesel Generator Building
  Performance Significance Determination Process. Under this SDP, record deficiencies
*Control Building Elevation 732 (Mechanical Equipment Room and Relay Room)  
  can be either minor or of very low safety significance (Green). This finding was
*Auxiliary Building Elevation 714 (Corridor)
  determined to be Green because it was related to the program for maintaining active
*Unit 2 Residual Heat Removal/Containment Spray Heat Exchanger RoomsThe inspectors observed the performance of the site fire brigade during unannounceddrills on March 29, 2006, and September 30, 23006, and reviewed the drill critique
  licenses and more than 20% of the records reviewed had deficiencies. (Section 1R11.3).
report for an unannounced drill on October 3, 2006, to evaluate the readiness of the fire
B. Licensee-Identified Violations
brigade to fight fires and to assess the drill against the requirements of the Sequoyah
  A violation of very low safety significance, which was identified by the licensee, was
Nuclear Plant Fire Protection Report, Revision 17. The observed drills simulated fires at
  reviewed by the inspectors. Corrective actions taken or planned by the licensee have
the 480-volt Reactor Motor Operated Valve Board 1B1-B and the Motor-driven Auxiliary
  been entered into the licensees corrective action program. This violation and corrective
Feedwater Pump 2A-A. The reviewed drill critique was for fire brigade response to a fire
  action are listed in Section 4OA7.
alarm report from the Unit 1 RWST. Specifically, the inspectors reviewed the following
                                                                                        Enclosure
aspects of the drills: use of protective clothing, use of breathing apparatus, proper use
 
of fire hoses, control of the drill scenario, and recurrence of identified deficiencies.   b.FindingsNo findings of significance were identified.1R07Heat Sink Performance   a.Inspection ScopeThe inspectors observed performance and reviewed the results of the following activityto verify the heat exchanger's readiness and availability. Inspector's interviewed
                                      REPORT DETAILS
maintenance and testing personnel and the system engineer, reviewed corrective action
      Summary of Plant Status:
program documents, previous heat exchanger flow rate data, and inspected the heat
      Unit 1 operated at or near 100% rated thermal power (RTP) for the duration of the
exchanger internals for cleanliness. Inspectors also walked down the system while in
      reporting period.
operation looking for evidence of leaks following system restoration. Documents
      Unit 2 operated at or near 100% RTP until November 27, 2006 when it shut down for a
reviewed are listed in the Attachment to this report. * WO 06-777564-000, Open 2B Containment Spray Heat Exchanger for EddyCurrent Inspection   b.FindingsNo findings of significance were identified.  
      refueling outage. Unit 2 achieved criticality on December 24, 2006, and reached 100%
6Enclosure1R08Inservice Inspection (ISI) Activities (71111.08).1Piping and Pressure Boundary Systems ISI    a.Inspection ScopeFrom December 4 - December 8, 2006, the inspectors observed and reviewed thelicensee's implementation of their ISI program for monitoring degradation of the reactor
      RTP on December 29, 2006, where it remained for the duration of the reporting period.
coolant system (RCS) boundary and other risk significant piping system boundaries for
1.   REACTOR SAFETY
Unit 2. The inspectors observed and reviewed a sample of American Society of
      Cornerstones: Initiating Events, Mitigating Systems, and Barrier Integrity
Mechanical Engineers (ASME), Section XI, Section III, and Risk Informed ISI required
1R01 Adverse Weather Protection
examinations, in order of risk priority, as identified in Section 71111.08-03 of inspection
   a. Inspection Scope
procedure 71111.08, "Inservice Inspection Activities" based upon the ISI activities
      The inspectors reviewed design features and licensee preparations for protecting the
available for review during the onsite inspection period.The inspectors conducted an on-site review of nondestructive examination (NDE)activities to evaluate compliance with TSs and the applicable editions of ASME Section
      essential raw cooling water (ERCW) intake structure and both Unit 1 and 2 refueling
V and Section XI to verify that indications and defects (if present) were appropriately
      water storage tanks (RWSTs) from extreme cold and freezing conditions. The
evaluated and dispositioned in accordance with the requirements of ASME Section XI
      inspectors reviewed the Updated Final Safety Analysis Report (UFSAR), and Technical
acceptance standards. The inspectors observed the following examinations:
      Specifications (TS), reviewed and observed implementation of licensee freeze protection
Manual Ultrasonic Examination:
      procedures, and walked down portions of the systems to assess the status of system
*13SIF-142
      deficiencies and the system readiness for extreme cold weather. Inspectors performed
Visual (VT3) examination of the following Hangers:
      corrective action program keyword searches to verify deficiencies were being identified
*2-CVCH-004*2-CVCH-007
      at an appropriate level and that actions were taken to correct problems. Documents
*2-CVCH-010
      reviewed are listed in the Attachment to this report.
*2-CVCH-037Qualification and certification records for examiners, inspection equipment, andconsumables along with the applicable NDE procedures for the above ISI examination
   b. Findings
activities were reviewed and compared to requirements stated in ASME Section V and
      No findings of significance were identified.
Section XI.The inspectors observed in-process welding activities for the following ASME pressureboundary locations. Inspectors reviewed quality records for welding procedures,
1R02 Evaluations of Changes, Tests or Experiments
procedure qualification, welder qualification, and filler metal certification. The inspectors observed a sample of in-process weld-overlay activities for the followingPressurizer nozzles:*Pressurizer Spray Nozzle*Pressurizer Surge Nozzle  
   a. Inspection Scope
7Enclosure   b.FindingsNo findings of significance were identified. .2Reactor Vessel Upper Head PenetrationsThe inspectors completed TI2515/150, Reactor Pressure Vessel Head and HeadPenetration Nozzles (NRC Order EA-03009) (Unit2), this outage. See Section 4OA5.2..3Boric Acid Corrosion Control (BACC) ISI    a.Inspection ScopeThe inspectors reviewed the licensee's BACC activities to ensure implementation withcommitments made in response to NRC Generic Letter 88-05 "Boric Acid Corrosion of
      The inspectors reviewed selected samples of 10 CFR 50.59 evaluations to verify that
Carbon Steel Reactor Pressure Boundary" and Bulletin 2002-01 "Reactor Pressure
      the licensee had appropriately considered the conditions under which changes to the
Vessel Head Degradation and Reactor Coolant Pressure Boundary Integrity." The inspectors conducted an on-site record review as well as an independent walkdownof parts of the reactor building that are not normally accessible during at-power
      facility, Updated Final Safety Analysis Report (UFSAR), or procedures may be made,
operations to evaluate compliance with licensee BACC program requirements. In
      and tests conducted, without prior NRC approval. The inspectors reviewed ten
particular, the inspectors assessed whether the visual examinations focused on
      evaluations completed for changes made by the licensee without prior NRC approval.
locations where boric acid leaks can cause degradation of safety significant components
      The inspectors also reviewed documents prepared in connection with the changes.
and that degraded or non-conforming conditions were properly identified in the
      Documents reviewed included supporting analyses, the UFSAR, and drawings to verify
licensee's corrective action program.The inspectors reviewed a sample of engineering evaluations completed for boric acidfound on reactor coolant system piping and components. The inspectors also reviewed
      that the licensee had correctly concluded that the changes could be made without
licensee corrective actions implemented for evidence of boric acid leakage to confirm
      obtaining a license amendment. The ten evaluations reviewed are listed in the
that they were consistent with requirements of Section XI of the ASME Code and 10
      Attachment to this report.
CFR 50 Appendix B Criterion XVI.     b. FindingsNo findings of significance were identified..4Steam Generator ISI    a.Inspection ScopeFrom December 11-15, 2006, the inspectors reviewed the Unit 2 Steam Generator (SG)tube eddy current testing (ECT) examination activities to ensure compliance with TSs,
                                                                                    Enclosure
applicable industry operating experience and technical guidance documents, and ASME
 
Code Section XI requirements.The inspectors reviewed licensee SG inspection activities to ensure that ECTinspections were conducted in accordance with the licensee's SG Program and
                                              4
applicable industry standards. The inspectors reviewed the SG examination scope,  
    Additionally, the inspectors reviewed samples of changes for which the licensee had
8EnclosureECT acquisition procedures, Examination Technique Specification Sheets (ETSS), ECTanalysis guidelines, the most recent SG degradation assessment and operational
    determined that evaluations were not required. The reviews were performed to verify
assessment, and also the condition monitoring results as they became available. The
    that the licensees conclusions to screen out these changes were correct, and the
inspectors reviewed documentation to ensure that the ECT probes and equipment
    changes were made in compliance with the requirements of 10 CFR 50.59. The sixteen
configurations used were qualified to detect the expected types of SG tube degradation.
    screened out changes reviewed are listed in the Attachment to this report.
The inspectors ensured that all tubes evaluated in condition monitoring were
    The inspectors also reviewed selected problem evaluation reports (PERs) to verify that
appropriately screened for in-situ testing. No tubes met the criteria for in-situ testing. In
    plant problems were evaluated for root/apparent causes; extent of condition; and that
addition, the inspectors ensured that the licensee had appropriately implemented the
    the developed corrective actions were adequate to ensure recurrence control of the
NRC-approved Alternate Repair Criteria (ARC) applicable to tubes that experienced
    identified plant problem.
outer diameter stress corrosion cracking (ODSCC) at tube support plates.The inspectors monitored the licensee's secondary side activities, which included aforeign object search and recovery (FOSAR) for loose parts, and sludge lancing. As
  b. Findings
part of an industry commitment, the licensee was required to remove a tube from
    No findings of significance were identified.
service for destructive testing. The inspectors monitored this evolution to ensure there
1R04 Equipment Alignment
was no damage to other tubes or other parts of the SG.    b. FindingsNo findings of significance were identified..5 Identification and Resolution of Problems    a.Inspection ScopeThe inspectors performed a review of piping system ISI related problems that wereidentified by the licensee and entered into the corrective action program. The inspectors
  a. Inspection Scope
reviewed corrective action documents to confirm that the licensee had appropriately
    Partial System Walkdowns. The inspectors performed a partial walkdown of the
described the scope of the problems. Additionally, the inspectors' review included
    following three systems to verify the operability of redundant or diverse trains and
confirmation that the licensee had an appropriate threshold for identifying issues and
    components when safety equipment was inoperable. The inspectors attempted to
had implemented effective corrective actions. The inspectors evaluated the threshold
    identify any discrepancies that could impact the function of the system, and, therefore,
for identifying issues through interviews with licensee staff and review of licensee
    potentially increase risk. The inspectors reviewed applicable operating procedures,
actions to incorporate lessons learned from industry issues related to the ISI program.  
    walked down control system components and verified that selected breakers, valves,
The inspectors performed these reviews to ensure compliance with 10 CFR Part 50, Appendix B, Criterion XVI, "Corrective Action," requirements. The corrective actiondocuments reviewed by the inspectors are listed in the Attachment to this report.    b. FindingsNo findings of significance were identified.  
    and support equipment were in the correct position to support system operation. The
9Enclosure1R11Licensed Operator Requalification Program.1Quarterly Inspection    a.Inspection ScopeThe inspectors observed licensed operator requalification simulator testing on October24, 2006. The testing involved a failed impulse pressure transmitter failure followed by
    inspectors also verified that the licensee had properly identified and resolved equipment
loss of condenser vacuum and automatic turbine trip. The reactor failed to automatically
    alignment problems that could cause initiating events or impact the capability of
trip and resulted in an anticipated transient without scram (ATWS). The ATWS was
    mitigating systems or barriers and entered them into the corrective action program.
compounded by the inability to trip the reactor from the Main Control Room, auxiliary
    Documents reviewed are listed in the Attachment to this report.
feedwater control valves failed to operate automatically for Steam Generators Number 1
    *       Residual Heat Removal (RHR) Train 2B during maintenance on Train 2A
and 2, and the Turbine Driven Auxiliary Feedwater Pump (TDAFP) was unable to supply
    *       Emergency Diesels 1A, 1B, and 2A during diesel 2B Outage
feedwater, all of which required operator action. As plant conditions were being
    *       Unit 2 Spent Fuel Pool Cooling during full core offload
stabilized, a pressurizer power operated relief valve (PORV) failed open and required
  b. Findings
operators to shut its blocking valve. The inspectors observed crew performance in terms of communications; ability to taketimely and proper actions; prioritizing, interpreting and verifying alarms; correct use and
    No findings of significance were identified.
implementation of procedures, including the alarm response procedures and emergency
1R05 Fire Protection
plan event classification; timely control board operation and manipulation, including highrisk operator actions; oversight and direction provided by shift manager, including the
  a. Inspection Scope
ability to identify and implement appropriate TS actions; independent event classification
    The inspectors conducted a tour of the eight areas listed below to assess the material
by the Shift Technical Advisor; and group dynamics involved in crew performance. The
    condition and operational status of fire protection features. The inspectors verified that
inspectors also observed the examining staff's assessment of the crew's performance
    combustibles and ignition sources were controlled in accordance with the licensees
and compared them to inspector observations. Documents reviewed are listed in the
    administrative procedures, fire detection and suppression equipment was available for
Attachment to this report.    b.FindingsNo findings of significance were identified..2Annual Review of Licensee Requalification Examination Results    a.Inspection ScopeOn November 17, 2006, the licensee completed the comprehensive requalificationbiennial written examinations and annual operating tests required to be given to alllicensed operators by 10 CFR 55.59(a)(2). The inspectors performed an in-office review
    use; that passive fire barriers were maintained in good material condition; and that
of the overall pass/fail results of the written examinations, individual operating tests, and
    compensatory measures for out-of-service, degraded, or inoperable fire protection
the crew simulator operating tests. These results were compared to the thresholds
                                                                                      Enclosure
established in Manual Chapter 609 Appendix I, Operator Requalification Human
 
Performance Significance Determination Process.    b.FindingsNo findings of significance were identified.  
                                                5
10Enclosure.3Licensed Operator Requalification Program - Biennial Review    a.Inspection ScopeThe inspectors reviewed facility operating history and associated documents inpreparation for this inspection. While onsite the inspectors reviewed documentation,
    equipment were implemented in accordance with the licensees fire plan. Documents
interviewed licensee personnel, and observed the administration of operating tests and
    reviewed are listed in the Attachment to this report.
written examinations associated with the licensee's operator requalification program.  
    *       Control Building Elevation 669 (Mechanical Equipment Room, 250-VDC Battery
Each of the activities performed by the inspectors was done to assess the effectiveness
              and Battery Board Rooms)
of the licensee in implementing requalification requirements identified in 10 CFR 55,
    *       Control Building Elevation 706 (Cable Spreading Room)
"Operators' Licenses.The evaluations were also performed to determine if the licensee
    *       Control Building Elevation 685 (Auxiliary Instrument Rooms)
effectively implemented operator requalification guidelines established in NUREG 1021,
    *       Auxiliary Building Elevation 690 (Corridor)
"Operator Licensing Examination Standards for Power Reactors," and Inspection
    *       Emergency Diesel Generator Building
Procedure 71111.11, "Licensed Operator Requalification Program.The inspectors also
    *       Control Building Elevation 732 (Mechanical Equipment Room and Relay Room)
evaluated the licensee's simulation facility for adequacy for use in operator licensing
    *       Auxiliary Building Elevation 714 (Corridor)
examinations using ANSI/ANS-3.5-1985, "American National Standard for Nuclear
    *       Unit 2 Residual Heat Removal/Containment Spray Heat Exchanger Rooms
Power Plant Simulators for use in Operator Training and Examination.The inspectors
    The inspectors observed the performance of the site fire brigade during unannounced
observed two crews during the performance of the operating tests. Documentation
    drills on March 29, 2006, and September 30, 23006, and reviewed the drill critique
reviewed included written examinations, job performance measures, simulator
    report for an unannounced drill on October 3, 2006, to evaluate the readiness of the fire
scenarios, licensee procedures, on-shift records, licensed operator qualification records,
    brigade to fight fires and to assess the drill against the requirements of the Sequoyah
watchstanding and medical records, simulator modification request records and
    Nuclear Plant Fire Protection Report, Revision 17. The observed drills simulated fires at
performance test records, the feedback process, and remediation plans.   Documents
    the 480-volt Reactor Motor Operated Valve Board 1B1-B and the Motor-driven Auxiliary
reviewed during the inspection are listed in the Attachment to this report.     b.FindingsIntroduction: A Green NCV was identified for failure to certify that the qualifications andstatus of licensed operators were current and valid prior to their resumption of license
    Feedwater Pump 2A-A. The reviewed drill critique was for fire brigade response to a fire
duties. The applicable requirements of 10 CFR 55.53, "Conditions of Licenses" for
    alarm report from the Unit 1 RWST. Specifically, the inspectors reviewed the following
license reactivation were not met. Specific aspects of the requalification program that
    aspects of the drills: use of protective clothing, use of breathing apparatus, proper use
were not valid included plant tours that were not completed with another licensed
    of fire hoses, control of the drill scenario, and recurrence of identified deficiencies.
operator and not completing all shift functions in the position to which the individual will
  b. Findings
be assigned. Description: The inspectors identified problems with several aspects of the reactivationprocess for licensed operators who had been reactivated between October 1, 2004 and
    No findings of significance were identified.
September 30, 2006. The inspectors performed a detailed review for 5 of the 15
1R07 Heat Sink Performance
individuals who had licenses reactivated during this time period. The inspectors identified that complete tours of the plant were not being conducted inaccordance with OPDP-1 "Operations Department Procedure", Revision 6 and 10 CFR
  a. Inspection Scope
55.53 requirements. Some individuals reactivating their licenses were performing the
    The inspectors observed performance and reviewed the results of the following activity
required plant tours without being accompanied by another licensed individual. The
    to verify the heat exchangers readiness and availability. Inspectors interviewed
inspectors also identified that some individuals reactivating their licenses had
    maintenance and testing personnel and the system engineer, reviewed corrective action
documented standing watch in non-TS positions, i.e., those positions that TSs do not
    program documents, previous heat exchanger flow rate data, and inspected the heat
require a licensed operator to fill. 10 CFR 55.53, requires that an authorized
    exchanger internals for cleanliness. Inspectors also walked down the system while in
representative of the facility certify that individuals reactivating their license must
    operation looking for evidence of leaks following system restoration. Documents
complete a minimum of 40 hours of shift functions in the position to which the individual  
    reviewed are listed in the Attachment to this report.
11Enclosurewill be assigned and under the direction of a reactor operator or senior reactor operatoras appropriate. The 40 hours shall also include a complete tour of the plant.The inspectors noted that the licensee performed a self assessment of the licensedoperator requalification program on September 11-26, 2006. The assessment identified
    *       WO 06-777564-000, Open 2B Containment Spray Heat Exchanger for Eddy
              Current Inspection
  b. Findings
    No findings of significance were identified.
                                                                                        Enclosure
 
                                                6
1R08 Inservice Inspection (ISI) Activities (71111.08)
.1    Piping and Pressure Boundary Systems ISI
   a. Inspection Scope
      From December 4 - December 8, 2006, the inspectors observed and reviewed the
      licensees implementation of their ISI program for monitoring degradation of the reactor
      coolant system (RCS) boundary and other risk significant piping system boundaries for
      Unit 2. The inspectors observed and reviewed a sample of American Society of
      Mechanical Engineers (ASME), Section XI, Section III, and Risk Informed ISI required
      examinations, in order of risk priority, as identified in Section 71111.08-03 of inspection
      procedure 71111.08, Inservice Inspection Activities based upon the ISI activities
      available for review during the onsite inspection period.
      The inspectors conducted an on-site review of nondestructive examination (NDE)
      activities to evaluate compliance with TSs and the applicable editions of ASME Section
      V and Section XI to verify that indications and defects (if present) were appropriately
      evaluated and dispositioned in accordance with the requirements of ASME Section XI
      acceptance standards.
      The inspectors observed the following examinations:
      Manual Ultrasonic Examination:
      *       13SIF-142
      Visual (VT3) examination of the following Hangers:
      *       2-CVCH-004
      *       2-CVCH-007
      *       2-CVCH-010
      *       2-CVCH-037
      Qualification and certification records for examiners, inspection equipment, and
      consumables along with the applicable NDE procedures for the above ISI examination
      activities were reviewed and compared to requirements stated in ASME Section V and
      Section XI.
      The inspectors observed in-process welding activities for the following ASME pressure
      boundary locations. Inspectors reviewed quality records for welding procedures,
      procedure qualification, welder qualification, and filler metal certification.
      The inspectors observed a sample of in-process weld-overlay activities for the following
      Pressurizer nozzles:
      *       Pressurizer Spray Nozzle
      *       Pressurizer Surge Nozzle
                                                                                        Enclosure
 
                                                7
   b. Findings
      No findings of significance were identified.
.2    Reactor Vessel Upper Head Penetrations
      The inspectors completed TI2515/150, Reactor Pressure Vessel Head and Head
      Penetration Nozzles (NRC Order EA-03009) (Unit2), this outage. See Section 4OA5.2.
.3    Boric Acid Corrosion Control (BACC) ISI
   a. Inspection Scope
      The inspectors reviewed the licensees BACC activities to ensure implementation with
      commitments made in response to NRC Generic Letter 88-05 Boric Acid Corrosion of
      Carbon Steel Reactor Pressure Boundary and Bulletin 2002-01 Reactor Pressure
      Vessel Head Degradation and Reactor Coolant Pressure Boundary Integrity.
      The inspectors conducted an on-site record review as well as an independent walkdown
      of parts of the reactor building that are not normally accessible during at-power
      operations to evaluate compliance with licensee BACC program requirements. In
      particular, the inspectors assessed whether the visual examinations focused on
      locations where boric acid leaks can cause degradation of safety significant components
      and that degraded or non-conforming conditions were properly identified in the
      licensees corrective action program.
      The inspectors reviewed a sample of engineering evaluations completed for boric acid
      found on reactor coolant system piping and components. The inspectors also reviewed
      licensee corrective actions implemented for evidence of boric acid leakage to confirm
      that they were consistent with requirements of Section XI of the ASME Code and 10
      CFR 50 Appendix B Criterion XVI.
  b. Findings
      No findings of significance were identified.
.4    Steam Generator ISI
   a. Inspection Scope
      From December 11-15, 2006, the inspectors reviewed the Unit 2 Steam Generator (SG)
      tube eddy current testing (ECT) examination activities to ensure compliance with TSs,
      applicable industry operating experience and technical guidance documents, and ASME
      Code Section XI requirements.
      The inspectors reviewed licensee SG inspection activities to ensure that ECT
      inspections were conducted in accordance with the licensees SG Program and
      applicable industry standards. The inspectors reviewed the SG examination scope,
                                                                                      Enclosure
 
                                                8
      ECT acquisition procedures, Examination Technique Specification Sheets (ETSS), ECT
      analysis guidelines, the most recent SG degradation assessment and operational
      assessment, and also the condition monitoring results as they became available. The
      inspectors reviewed documentation to ensure that the ECT probes and equipment
      configurations used were qualified to detect the expected types of SG tube degradation.
      The inspectors ensured that all tubes evaluated in condition monitoring were
      appropriately screened for in-situ testing. No tubes met the criteria for in-situ testing. In
      addition, the inspectors ensured that the licensee had appropriately implemented the
      NRC-approved Alternate Repair Criteria (ARC) applicable to tubes that experienced
      outer diameter stress corrosion cracking (ODSCC) at tube support plates.
      The inspectors monitored the licensees secondary side activities, which included a
      foreign object search and recovery (FOSAR) for loose parts, and sludge lancing. As
      part of an industry commitment, the licensee was required to remove a tube from
      service for destructive testing. The inspectors monitored this evolution to ensure there
      was no damage to other tubes or other parts of the SG.
   b. Findings
      No findings of significance were identified.
.5   Identification and Resolution of Problems
   a. Inspection Scope
      The inspectors performed a review of piping system ISI related problems that were
      identified by the licensee and entered into the corrective action program. The inspectors
      reviewed corrective action documents to confirm that the licensee had appropriately
      described the scope of the problems. Additionally, the inspectors review included
      confirmation that the licensee had an appropriate threshold for identifying issues and
      had implemented effective corrective actions. The inspectors evaluated the threshold
      for identifying issues through interviews with licensee staff and review of licensee
      actions to incorporate lessons learned from industry issues related to the ISI program.
      The inspectors performed these reviews to ensure compliance with 10 CFR Part 50,
      Appendix B, Criterion XVI, Corrective Action, requirements. The corrective action
      documents reviewed by the inspectors are listed in the Attachment to this report.
   b. Findings
      No findings of significance were identified.
                                                                                        Enclosure
 
                                                  9
1R11 Licensed Operator Requalification Program
.1    Quarterly Inspection
   a. Inspection Scope
      The inspectors observed licensed operator requalification simulator testing on October
      24, 2006. The testing involved a failed impulse pressure transmitter failure followed by
      loss of condenser vacuum and automatic turbine trip. The reactor failed to automatically
      trip and resulted in an anticipated transient without scram (ATWS). The ATWS was
      compounded by the inability to trip the reactor from the Main Control Room, auxiliary
      feedwater control valves failed to operate automatically for Steam Generators Number 1
      and 2, and the Turbine Driven Auxiliary Feedwater Pump (TDAFP) was unable to supply
      feedwater, all of which required operator action. As plant conditions were being
      stabilized, a pressurizer power operated relief valve (PORV) failed open and required
      operators to shut its blocking valve.
      The inspectors observed crew performance in terms of communications; ability to take
      timely and proper actions; prioritizing, interpreting and verifying alarms; correct use and
      implementation of procedures, including the alarm response procedures and emergency
      plan event classification; timely control board operation and manipulation, including high
      risk operator actions; oversight and direction provided by shift manager, including the
      ability to identify and implement appropriate TS actions; independent event classification
      by the Shift Technical Advisor; and group dynamics involved in crew performance. The
      inspectors also observed the examining staffs assessment of the crews performance
      and compared them to inspector observations. Documents reviewed are listed in the
      Attachment to this report.
   b. Findings
      No findings of significance were identified.
.2    Annual Review of Licensee Requalification Examination Results
   a. Inspection Scope
      On November 17, 2006, the licensee completed the comprehensive requalification
      biennial written examinations and annual operating tests required to be given to all
      licensed operators by 10 CFR 55.59(a)(2). The inspectors performed an in-office review
      of the overall pass/fail results of the written examinations, individual operating tests, and
      the crew simulator operating tests. These results were compared to the thresholds
      established in Manual Chapter 609 Appendix I, Operator Requalification Human
      Performance Significance Determination Process.
   b. Findings
      No findings of significance were identified.
                                                                                          Enclosure
 
                                                  10
.3    Licensed Operator Requalification Program - Biennial Review
   a. Inspection Scope
      The inspectors reviewed facility operating history and associated documents in
      preparation for this inspection. While onsite the inspectors reviewed documentation,
      interviewed licensee personnel, and observed the administration of operating tests and
      written examinations associated with the licensees operator requalification program.
      Each of the activities performed by the inspectors was done to assess the effectiveness
      of the licensee in implementing requalification requirements identified in 10 CFR 55,
      Operators Licenses. The evaluations were also performed to determine if the licensee
      effectively implemented operator requalification guidelines established in NUREG 1021,
      Operator Licensing Examination Standards for Power Reactors, and Inspection
      Procedure 71111.11, Licensed Operator Requalification Program. The inspectors also
      evaluated the licensees simulation facility for adequacy for use in operator licensing
      examinations using ANSI/ANS-3.5-1985, American National Standard for Nuclear
      Power Plant Simulators for use in Operator Training and Examination. The inspectors
      observed two crews during the performance of the operating tests. Documentation
      reviewed included written examinations, job performance measures, simulator
      scenarios, licensee procedures, on-shift records, licensed operator qualification records,
      watchstanding and medical records, simulator modification request records and
      performance test records, the feedback process, and remediation plans. Documents
      reviewed during the inspection are listed in the Attachment to this report.
  b. Findings
      Introduction: A Green NCV was identified for failure to certify that the qualifications and
      status of licensed operators were current and valid prior to their resumption of license
      duties. The applicable requirements of 10 CFR 55.53, Conditions of Licenses for
      license reactivation were not met. Specific aspects of the requalification program that
      were not valid included plant tours that were not completed with another licensed
      operator and not completing all shift functions in the position to which the individual will
      be assigned.
      Description: The inspectors identified problems with several aspects of the reactivation
      process for licensed operators who had been reactivated between October 1, 2004 and
      September 30, 2006. The inspectors performed a detailed review for 5 of the 15
      individuals who had licenses reactivated during this time period.
      The inspectors identified that complete tours of the plant were not being conducted in
      accordance with OPDP-1 Operations Department Procedure, Revision 6 and 10 CFR
      55.53 requirements. Some individuals reactivating their licenses were performing the
      required plant tours without being accompanied by another licensed individual. The
      inspectors also identified that some individuals reactivating their licenses had
      documented standing watch in non-TS positions, i.e., those positions that TSs do not
      require a licensed operator to fill. 10 CFR 55.53, requires that an authorized
      representative of the facility certify that individuals reactivating their license must
      complete a minimum of 40 hours of shift functions in the position to which the individual
                                                                                          Enclosure
 
                                          11
will be assigned and under the direction of a reactor operator or senior reactor operator
as appropriate. The 40 hours shall also include a complete tour of the plant.
The inspectors noted that the licensee performed a self assessment of the licensed
operator requalification program on September 11-26, 2006. The assessment identified
problems in several different areas related to operator license reactivation and
problems in several different areas related to operator license reactivation and
maintenance of active license process. Specifically, one licensed operator's reactivationdocuments could not be located, two licensed operators were returned to active status
maintenance of active license process. Specifically, one licensed operators reactivation
documents could not be located, two licensed operators were returned to active status
without all required training completed, and one inactive licensed operator assumed
without all required training completed, and one inactive licensed operator assumed
licensed duties without being reactivated. Analysis: The inspectors determined that the licensee's failure to properly certify andmaintain the reactivation records of licensed operators and the failure to perform plant
licensed duties without being reactivated.
Analysis: The inspectors determined that the licensees failure to properly certify and
maintain the reactivation records of licensed operators and the failure to perform plant
tours with another licensed operator and complete shift functions in the position to which
tours with another licensed operator and complete shift functions in the position to which
the individual will be assigned is a performance deficiency because the licensee must
the individual will be assigned is a performance deficiency because the licensee must
satisfy the requirements of 10 CFR 55.53 for license reactivation.The finding is more than minor because it is associated with the human performance attribute of the Mitigating Systems Cornerstone and adversely affects the cornerstone
satisfy the requirements of 10 CFR 55.53 for license reactivation.
The finding is more than minor because it is associated with the human performance
attribute of the Mitigating Systems Cornerstone and adversely affects the cornerstone
objective of ensuring the availability, reliability, and capability of operators to response to
objective of ensuring the availability, reliability, and capability of operators to response to
initiating events to prevent undesirable consequences. The failure to properly reactivate
initiating events to prevent undesirable consequences. The failure to properly reactivate
the licenses of operators could adversely impact their performance. The finding was
the licenses of operators could adversely impact their performance. The finding was
evaluated using the Operator Requalification Human Performance Significance
evaluated using the Operator Requalification Human Performance Significance
Determination Process. Under this SDP, record deficiencies can be either minor or of
Determination Process. Under this SDP, record deficiencies can be either minor or of
very low safety significance (Green). This finding was determined to be Green because
very low safety significance (Green). This finding was determined to be Green because
it was related to the program for maintaining active licenses and more than 20% of the
it was related to the program for maintaining active licenses and more than 20% of the
records reviewed had deficiencies.Enforcement: 10 CFR 55.53.(f) "Conditions of Licenses" requires, in part, that anauthorized representative of the facility licensee shall certify that qualifications and
records reviewed had deficiencies.
Enforcement: 10 CFR 55.53.(f) Conditions of Licenses requires, in part, that an
authorized representative of the facility licensee shall certify that qualifications and
status of operator licensees are current and valid prior to the resumption of license
status of operator licensees are current and valid prior to the resumption of license
duties. Included in the certification required by 10 CRF 55.53 is that the individual
duties. Included in the certification required by 10 CRF 55.53 is that the individual
complete a minimum of 40 hours of shift functions in the position to be assigned and
complete a minimum of 40 hours of shift functions in the position to be assigned and
also complete a plant tour while accompanied by a licensed operator. Contrary to the
also complete a plant tour while accompanied by a licensed operator. Contrary to the
above, the licensee did not properly certify that qualifications and status were current
above, the licensee did not properly certify that qualifications and status were current
and valid prior to allowing operators to perform licensed duties. The failure to properly reactivate licensed operators was determined to be of very lowsafety significance (Green) and has been entered into the licensee's corrective action
and valid prior to allowing operators to perform licensed duties.
program as PER No.112004. The finding is being treated as an NCV consistent with
The failure to properly reactivate licensed operators was determined to be of very low
safety significance (Green) and has been entered into the licensees corrective action
program as PER No.112004. The finding is being treated as an NCV consistent with
Section VI.A of the NRC Enforcement Policy: NCV 05000327,328/2006005-01, Failure
Section VI.A of the NRC Enforcement Policy: NCV 05000327,328/2006005-01, Failure
to certify qualifications and status of licensed operators were current and valid in
to certify qualifications and status of licensed operators were current and valid in
accordance with 10CFR 55.53.  
accordance with 10CFR 55.53.
12Enclosure1R12Maintenance Effectiveness   a.Inspection ScopeThe inspectors reviewed the following three maintenance activities to verify theeffectiveness of the activities in terms of: 1) appropriate work practices; 2) identifying
                                                                                      Enclosure
and addressing common cause failures; 3) scoping in accordance with 10 CFR 50.65
 
(b); 4) characterizing reliability issues for performance; 5) trending key parameters for
                                                12
condition monitoring; 6) charging unavailability for performance; 7) classification in
1R12 Maintenance Effectiveness
accordance with 10 CFR 50.65(a)(1) or (a)(2); 8) appropriateness of performance
  a. Inspection Scope
criteria for Systems, Structures, and Components (SSCs) and functions classified as
    The inspectors reviewed the following three maintenance activities to verify the
(a)(2); and 9) appropriateness of goals and corrective actions for SSCs and functions
    effectiveness of the activities in terms of: 1) appropriate work practices; 2) identifying
classified as (a)(1). Documents reviewed are listed in the Attachment to this report.   *PER 115421, B-B Main Control Room Ventilation *PER 115780, 2B Residual Heat Removal HX Outlet Valve 74-28 Failure  
    and addressing common cause failures; 3) scoping in accordance with 10 CFR 50.65
*PER 85481, Repeated Packing Leaks of Safety Injection (SI) Valve 2-FCV-63-156   b.FindingsNo findings of significance were identified.1R13Maintenance Risk Assessments and Emergent Work Control   a.Inspection ScopeThe inspectors reviewed the following six activities to verify that the appropriate riskassessments were performed prior to removing equipment from service for
    (b); 4) characterizing reliability issues for performance; 5) trending key parameters for
maintenance. The inspectors verified that risk assessments were performed as
    condition monitoring; 6) charging unavailability for performance; 7) classification in
required by 10 CFR 50.65 (a)(4), and were accurate and complete. When emergent
    accordance with 10 CFR 50.65(a)(1) or (a)(2); 8) appropriateness of performance
work was performed, the inspectors verified that the plant risk was promptly reassessed
    criteria for Systems, Structures, and Components (SSCs) and functions classified as
and managed. The inspectors verified the appropriate use of the licensee's risk
    (a)(2); and 9) appropriateness of goals and corrective actions for SSCs and functions
assessment tool and risk categories in accordance with Procedure SPP-7.1, On-Line
    classified as (a)(1). Documents reviewed are listed in the Attachment to this report.
Work Management, Revision 8, and Instruction 0-TI-DSM-000-007.1, Risk Assessment
    *       PER 115421, B-B Main Control Room Ventilation
Guidelines, Revision 8. Documents reviewed are listed in the Attachment to this report. *Unit 2 ECCS Train A Room Cooler Outage*Unplanned EDG 2B Inoperability
    *       PER 115780, 2B Residual Heat Removal HX Outlet Valve 74-28 Failure
*2-SI-OPS-082-26A, Loss of Offsite Power with SI - DG 2A-A Test, Revision 35  
    *       PER 85481, Repeated Packing Leaks of Safety Injection (SI) Valve 2-FCV-63-156
*ORAM Orange risk condition from Unit 2 midloop activities prior to vacuum refill
  b. Findings
*Franklin 500KV line tripped resulting in Technical Specification 3.8.1.1 entry
    No findings of significance were identified.
*Unit 2 initial RCS level drain to partial draindown condition   b.FindingsNo findings of significance were identified.  
1R13 Maintenance Risk Assessments and Emergent Work Control
13Enclosure1R15Operability Evaluations   a.Inspection ScopeFor the five operability evaluations described in the PERs listed below, the inspectorsevaluated the technical adequacy of the evaluations to ensure that TS operability was
  a. Inspection Scope
properly justified and the subject component or system remained available, such that no
    The inspectors reviewed the following six activities to verify that the appropriate risk
unrecognized increase in risk occurred. The inspectors reviewed the UFSAR to verify
    assessments were performed prior to removing equipment from service for
that the system or component remained available to perform its intended function. In
    maintenance. The inspectors verified that risk assessments were performed as
addition, the inspectors reviewed compensatory measures implemented to verify that
    required by 10 CFR 50.65 (a)(4), and were accurate and complete. When emergent
the compensatory measures worked as stated and the measures were adequately
    work was performed, the inspectors verified that the plant risk was promptly reassessed
controlled. The inspectors also reviewed a sampling of PERs to verify that the licensee
    and managed. The inspectors verified the appropriate use of the licensees risk
was identifying and correcting any deficiencies associated with operability evaluations.  
    assessment tool and risk categories in accordance with Procedure SPP-7.1, On-Line
Documents reviewed are listed in the Attachment to this report.*PER 111814, Train 'A' MCR Air-Conditioning System Air Flow Greater ThanAcceptance Criteria*PERs 114769, 114941, Emergency Diesel Generator 2B Feeder Breaker Failedto Close When Required *PER 109326, ERCW Screen Wash Pump B-B Failed Pump Performance Test
    Work Management, Revision 8, and Instruction 0-TI-DSM-000-007.1, Risk Assessment
*PER 115490, Charging Pump Discharge Manual Isolation Valve Appendix ROperability*PER 117113, Unit 1 Steam Generator Levels Exhibited Lowering Trend   b.FindingsNo findings of significance were identified. An unresolved item (URI) is discussedbelow.Inability to Perform Actions Required by AOP-N.08, Appendix R Fire Safe ShutdownIntroduction: The inspectors identified an Unresolved Item (URI) for not promptlyidentifying and correcting problems associated with manual valve 2-62-527. These
    Guidelines, Revision 8. Documents reviewed are listed in the Attachment to this report.
problems resulted in operators not being able to comply with licensee procedure AOP-
    *       Unit 2 ECCS Train A Room Cooler Outage
N.08, Appendix R Fire Safe Shutdown due to manual valve 2-62-527 not being able to
    *       Unplanned EDG 2B Inoperability
be closed within the 13 minutes required.Description: On October 28, 2005, a procedure change to AOP-N.08, Appendix R FireSafe Shutdown, was implemented. This change incorporated updated guidance
    *       2-SI-OPS-082-26A, Loss of Offsite Power with SI - DG 2A-A Test, Revision 35
provided by a Westinghouse technical bulletin (TB -04-022) concerning RCP seal
    *       ORAM Orange risk condition from Unit 2 midloop activities prior to vacuum refill
performance during Appendix R fires and a loss of all pump seal cooling. This change
    *       Franklin 500KV line tripped resulting in Technical Specification 3.8.1.1 entry
reduced the time available to perform manual actions and restore RCP seal flow from 24
    *       Unit 2 initial RCS level drain to partial draindown condition
minutes to 13 minutes. In the event of an Appendix R fire resulting in a spurious safety
  b. Findings
injection signal, plant procedures required that all RCS injection sources be stopped to
    No findings of significance were identified.
prevent filling the pressurizer solid. The vendor guidance stated that actions taken to
                                                                                        Enclosure
prevent this condition and restore RCP seal flow should be completed within 13 minutes
 
to prevent seal damage. The actions outlined by AOP-N.08 required an auxiliary unit
                                              13
operator (AUO) to manipulate several valves in the appropriate Charging Pump room  
1R15 Operability Evaluations
14Enclosureand then a CCP restarted to restore seal flow. Specifically, the AUO was to open adedicated flow path to the RCP seals using manual valve 62-526 (A-train), or 62-534 (B-
  a. Inspection Scope
    For the five operability evaluations described in the PERs listed below, the inspectors
    evaluated the technical adequacy of the evaluations to ensure that TS operability was
    properly justified and the subject component or system remained available, such that no
    unrecognized increase in risk occurred. The inspectors reviewed the UFSAR to verify
    that the system or component remained available to perform its intended function. In
    addition, the inspectors reviewed compensatory measures implemented to verify that
    the compensatory measures worked as stated and the measures were adequately
    controlled. The inspectors also reviewed a sampling of PERs to verify that the licensee
    was identifying and correcting any deficiencies associated with operability evaluations.
    Documents reviewed are listed in the Attachment to this report.
    *       PER 111814, Train A MCR Air-Conditioning System Air Flow Greater Than
              Acceptance Criteria
    *       PERs 114769, 114941, Emergency Diesel Generator 2B Feeder Breaker Failed
              to Close When Required
    *       PER 109326, ERCW Screen Wash Pump B-B Failed Pump Performance Test
    *       PER 115490, Charging Pump Discharge Manual Isolation Valve Appendix R
              Operability
    *       PER 117113, Unit 1 Steam Generator Levels Exhibited Lowering Trend
  b. Findings
    No findings of significance were identified. An unresolved item (URI) is discussed
    below.
    Inability to Perform Actions Required by AOP-N.08, Appendix R Fire Safe Shutdown
    Introduction: The inspectors identified an Unresolved Item (URI) for not promptly
    identifying and correcting problems associated with manual valve 2-62-527. These
    problems resulted in operators not being able to comply with licensee procedure AOP-
    N.08, Appendix R Fire Safe Shutdown due to manual valve 2-62-527 not being able to
    be closed within the 13 minutes required.
    Description: On October 28, 2005, a procedure change to AOP-N.08, Appendix R Fire
    Safe Shutdown, was implemented. This change incorporated updated guidance
    provided by a Westinghouse technical bulletin (TB -04-022) concerning RCP seal
    performance during Appendix R fires and a loss of all pump seal cooling. This change
    reduced the time available to perform manual actions and restore RCP seal flow from 24
    minutes to 13 minutes. In the event of an Appendix R fire resulting in a spurious safety
    injection signal, plant procedures required that all RCS injection sources be stopped to
    prevent filling the pressurizer solid. The vendor guidance stated that actions taken to
    prevent this condition and restore RCP seal flow should be completed within 13 minutes
    to prevent seal damage. The actions outlined by AOP-N.08 required an auxiliary unit
    operator (AUO) to manipulate several valves in the appropriate Charging Pump room
                                                                                      Enclosure
 
                                        14
and then a CCP restarted to restore seal flow. Specifically, the AUO was to open a
dedicated flow path to the RCP seals using manual valve 62-526 (A-train), or 62-534 (B-
train) and close the associated CCP manual discharge valve, 62-527 (A-train) or 62-533
train) and close the associated CCP manual discharge valve, 62-527 (A-train) or 62-533
(B-train) to the CCP Injection Tank (CCPIT). To support the procedure change, these
(B-train) to the CCP Injection Tank (CCPIT). To support the procedure change, these
manipulations were subjected to a manual action validation that consisted of a table top
manipulations were subjected to a manual action validation that consisted of a table top
review of the necessary steps. The licensee determined that the CCP manual
review of the necessary steps. The licensee determined that the CCP manual
discharge valves to the CCPIT could be closed by an individual AUO in 5 minutes and
discharge valves to the CCPIT could be closed by an individual AUO in 5 minutes and
 
20 seconds.
20 seconds.Prior to the procedure being approved, PER 91383 was written on October 24, 2005. The PER addressed concerns by at least one plant AUO that the manual actions
Prior to the procedure being approved, PER 91383 was written on October 24, 2005.
The PER addressed concerns by at least one plant AUO that the manual actions
required by the change to procedure AOP-N.08 may not be able to be completed within
required by the change to procedure AOP-N.08 may not be able to be completed within
the time required. PER 91383 requested the need to further evaluate the time
the time required. PER 91383 requested the need to further evaluate the time
necessary to perform the manual actions by actual valve manipulations, or whether
necessary to perform the manual actions by actual valve manipulations, or whether
additional procedure changes were needed to provide more margin to the required time.  
additional procedure changes were needed to provide more margin to the required time.
The corrective action planned was to perform a timed valve stroke of CCP discharge
The corrective action planned was to perform a timed valve stroke of CCP discharge
valve 2-62-527 to validate procedural change assumptions. Work Order (WO) 06-
valve 2-62-527 to validate procedural change assumptions. Work Order (WO) 06-
771729-000 was written to implement and track this action during an appropriate CCP
771729-000 was written to implement and track this action during an appropriate CCP
maintenance period. PER 91383 was closed as completed on February 24, 2006 based
maintenance period. PER 91383 was closed as completed on February 24, 2006 based
on the WO being written. On November 9, 2006, during a self-assessment, the licensee
on the WO being written. On November 9, 2006, during a self-assessment, the licensee
determined that the WO had not been completed and was not scheduled for
determined that the WO had not been completed and was not scheduled for
performance until January 22, 2007. PER 114455 was written to document the
performance until January 22, 2007. PER 114455 was written to document the
incomplete corrective action. Upon review of PER 114455, the inspectors questioned
incomplete corrective action. Upon review of PER 114455, the inspectors questioned
the licensee on the valve's history, the status of corrective actions, and whether a valid
the licensee on the valves history, the status of corrective actions, and whether a valid
safety concern existed if the valve could not be operated within the prescribed time.  
safety concern existed if the valve could not be operated within the prescribed time.
Prior to resolution by the licensee, on November 27, 2006, during Unit 2 refueling
Prior to resolution by the licensee, on November 27, 2006, during Unit 2 refueling
outage activities, operators closed valve 2-62-527 to support maintenance. The
outage activities, operators closed valve 2-62-527 to support maintenance. The
operators reported that the valve was very difficult to operate and required
operators reported that the valve was very difficult to operate and required
approximately 30 minutes for two AUOs to shut the valve. This observation was
approximately 30 minutes for two AUOs to shut the valve. This observation was
documented in in PER 115490 and supported the initial concern expressed in PER
documented in in PER 115490 and supported the initial concern expressed in PER
91383. This information prompted the license to evaluate the consequences of the additionaltime needed to operate valve 2-62-527 with plant Appendix R procedures. Functional
91383.
This information prompted the license to evaluate the consequences of the additional
time needed to operate valve 2-62-527 with plant Appendix R procedures. Functional
Evaluation (FE) 41722 was drafted and the licensee determined that RCP seal
Evaluation (FE) 41722 was drafted and the licensee determined that RCP seal
degradation would not occur if RCP seal flow was restored with a CCP prior to
degradation would not occur if RCP seal flow was restored with a CCP prior to
completing of the Appendix R Fire safe shutdown manual actions The licensee also
completing of the Appendix R Fire safe shutdown manual actions The licensee also
evaluated whether the same problems were likely for other Appendix R manual valves. .
evaluated whether the same problems were likely for other Appendix R manual valves. .
The licensee drafted a document to support the determination that other valves in both
The licensee drafted a document to support the determination that other valves in both
units could be operated in adequate time in the event of an Appendix R fire.        
units could be operated in adequate time in the event of an Appendix R fire.
Analysis: The inspectors determined that the delay in implementing the WO resulted innot promptly identifying and correcting problems with manual valve 2-62-527 resulting in
Analysis: The inspectors determined that the delay in implementing the WO resulted in
not promptly identifying and correcting problems with manual valve 2-62-527 resulting in
operators not being able to comply with procedure AOP-N.08, Appendix R Fire Safe
operators not being able to comply with procedure AOP-N.08, Appendix R Fire Safe
Shutdown. The corrective action for PER 91383 was closed to a WO and rescheduled
Shutdown. The corrective action for PER 91383 was closed to a WO and rescheduled
several times in the work control process with a performance date of January 22, 2007.  
several times in the work control process with a performance date of January 22, 2007.
The inspectors referenced Inspection Manual Chapter (IMC) 0612 and determined the
The inspectors referenced Inspection Manual Chapter (IMC) 0612 and determined the
finding is more than minor because if left uncorrected, the licensee would not be able to  
finding is more than minor because if left uncorrected, the licensee would not be able to
15Enclosurecomply with AOP-N.08. The finding is associated with the mitigating systemcornerstone and could be reasonably viewed as affecting the cornerstone objective to
                                                                                Enclosure
ensure the availability, reliability, and capability of systems that respond to initiating
 
events to prevent undesirable consequences. This finding is unresolved pending the
                                                15
review of supporting documentation and completion of the significance determination. Enforcement: Pending additional information involving the circumstances surroundingthe event, its extent of condition and completion of the significance determination, this
    comply with AOP-N.08. The finding is associated with the mitigating system
finding is identified as URI 05000328/2006005-02, Inability to Perform Required Actions
    cornerstone and could be reasonably viewed as affecting the cornerstone objective to
of AOP-N.08, Appendix R Fire Safe Shutdown.1R17Permanent Plant Modifications   a.Inspection ScopeThe inspectors performed independent design reviews of six plant modifications in theInitiating Events, Mitigating Systems, and Barrier Integrity cornerstone areas, to verify
    ensure the availability, reliability, and capability of systems that respond to initiating
that the plant modifications did not have any adverse effects on system availability,
    events to prevent undesirable consequences. This finding is unresolved pending the
reliability, and functional capability. Documents reviewed included procedures,
    review of supporting documentation and completion of the significance determination.
engineering calculations, modification design and implementation packages, work
    Enforcement: Pending additional information involving the circumstances surrounding
orders, Condition Reports (CRs), applicable sections of the UFSAR, TSs, and design
    the event, its extent of condition and completion of the significance determination, this
basis information. The plant modifications and the associated attributes reviewed are as
    finding is identified as URI 05000328/2006005-02, Inability to Perform Required Actions
follows: DCN D22050, Pressurizer Relief Tank Level Transmitter Removed (Barrier Integrity)*Control Signal
    of AOP-N.08, Appendix R Fire Safe Shutdown.
*Energy Needs
1R17 Permanent Plant Modifications
*Process Medium
  a. Inspection Scope
*Update of Licensee DocumentsDCN D21781, Change Steam Generator Narrow Range Level Transmitter Scaling(Mitigating System)
    The inspectors performed independent design reviews of six plant modifications in the
*Control Signal
    Initiating Events, Mitigating Systems, and Barrier Integrity cornerstone areas, to verify
*Energy Needs
    that the plant modifications did not have any adverse effects on system availability,
*Process Medium
    reliability, and functional capability. Documents reviewed included procedures,
*Update of Licensee Documents
    engineering calculations, modification design and implementation packages, work
*OperationsDCN D21911, Replace Containment Isolation Valve 2-FCV-030-0014(Barrier Integrity)*Pressure Boundary
    orders, Condition Reports (CRs), applicable sections of the UFSAR, TSs, and design
*Structural
    basis information. The plant modifications and the associated attributes reviewed are as
*Process Medium
    follows:
*Update of Licensee Documents
    DCN D22050, Pressurizer Relief Tank Level Transmitter Removed (Barrier Integrity)
*Materials/Replacement ComponentsDCN 21900, Replace Unit 1B Main Bank Transformer and Associated Fire ProtectionRing Header, Revision A.(Initiating Event)
    *         Control Signal
*Energy Needs
    *         Energy Needs
*Control Signals
    *         Process Medium
*Post-Installation Testing  
    *         Update of Licensee Documents
16Enclosure*Update of Licensee Documents*Functional Testing Adequacy and ResultsDCN D21971, Replace Cable PP351A for D/G 1A-A, Revision A. (Mitigating Systems)*Materials/ Replacement
    DCN D21781, Change Steam Generator Narrow Range Level Transmitter Scaling
*Failure Modes
    (Mitigating System)
*Post-Installation Testing
    *         Control Signal
*Update of Licensee Documents
    *         Energy Needs
*Functional Testing Adequacy and ResultsDCN D21827, Revise Setting on Raw Cooling Water Pump Breaker, Revision A.*Control Signals
    *         Process Medium
*Response Time
    *         Update of Licensee Documents
*Post-Insulation Testing
    *         Operations
*Update of Licensee Documents
    DCN D21911, Replace Containment Isolation Valve 2-FCV-030-0014(Barrier Integrity)
*Functional Testing Adequacy and ResultsThe inspectors also performed field inspections of selected plant modifications to verifythat the as-built installation complied with design requirements delineated in approved
    *         Pressure Boundary
design documents. Additionally, the inspectors reviewed selected PERs to verify that
    *         Structural
plant problems were evaluated for root/apparent causes, extent of condition, and that
    *         Process Medium
the developed corrective actions were adequate to ensure recurrence control of the
    *         Update of Licensee Documents
identified plant problem.     b.FindingsNo findings of significance were identified.1R19Post-Maintenance Testing   a.Inspection ScopeThe inspectors reviewed the five post-maintenance tests listed below to verify thatprocedures and test activities ensured system operability and functional capability. The
    *         Materials/Replacement Components
inspectors reviewed the licensee's test procedure to verify that the procedure
    DCN 21900, Replace Unit 1B Main Bank Transformer and Associated Fire Protection
adequately tested the safety function(s) that may have been affected by the
    Ring Header, Revision A.(Initiating Event)
maintenance activity, that the acceptance criteria in the procedure were consistent with
    *         Energy Needs
information in the applicable licensing basis and/or design basis documents, and that
    *         Control Signals
the procedure had been properly reviewed and approved. The inspectors also
    *         Post-Installation Testing
witnessed the test or reviewed the test data, to verify that test results adequately
                                                                                          Enclosure
demonstrated restoration of the affected safety function(s). Documents reviewed are
 
listed in the Attachment to this report.*WO 05-782379-000, Breaker Changeout for Motor-driven Auxiliary Feedwater(AFW) Pump 2B*2-SI-OPS-000-009.0, Actuation of Emergency Core Cooling Systems (ECCS)and Boron Injection Flowpath Valves Via SI Signal, Revision 1*WO 05-777912-001, Repack SI system Hot Leg Injection Valve, 2-FCV-63-156  
                                              16
17Enclosure*WO 06-780773-000, Calibrate FCV and Limit Switches on 2-FCV-074-28 *2-SI-SLT-088-156.0, Containment Integrated Leak Rate Test, Revision 2   b.FindingsNo findings of significance were identified.1R20Refueling and Other Outage Activities   a.Inspection ScopeFor the Unit 2 refueling outage that began on November 27, 2006, the inspectorsevaluated licensee activities to verify that the licensee considered risk in developing
    *       Update of Licensee Documents
outage schedules, followed risk reduction methods developed to control plant
    *       Functional Testing Adequacy and Results
configuration, developed mitigation strategies for the loss of key safety functions, and
    DCN D21971, Replace Cable PP351A for D/G 1A-A, Revision A. (Mitigating Systems)
adhered to operating license and TS requirements that ensure defense-in-depth. The
    *       Materials/ Replacement
inspectors also walked down portions of Unit 2 not normally accessible during at-power
    *       Failure Modes
operations to verify that safety-related and risk-significant SSCs were maintained in an
    *       Post-Installation Testing
operable condition. Specifically, between November 27, 2006, and December 26, 2006,
    *       Update of Licensee Documents
the inspectors performed inspections and reviews of the following outage activities.  
    *       Functional Testing Adequacy and Results
Documents reviewed are listed in the Attachment to this report.*Outage Plan. The inspectors reviewed the outage safety plan and contingencyplans to confirm that the licensee had appropriately considered risk, industry
    DCN D21827, Revise Setting on Raw Cooling Water Pump Breaker, Revision A.
experience, and previous site-specific problems in developing and implementing
    *       Control Signals
a plan that assured maintenance of defense-in-depth.*Reactor Shutdown. The inspectors observed the shutdown in the control roomfrom the time the reactor was tripped until operators placed it on the RHR
    *       Response Time
system for decay heat removal to verify that TS cooldown restrictions were
    *       Post-Insulation Testing
followed. The inspectors also toured the lower containment as soon as
    *       Update of Licensee Documents
practicable after reactor shutdown to observe the general condition of the RCS
    *       Functional Testing Adequacy and Results
and emergency core cooling system components and to look for indications of
    The inspectors also performed field inspections of selected plant modifications to verify
previously unidentified leakage inside the polar crane wall.*Licensee Control of Outage Activities. On a daily basis, the inspectors attendedthe licensee outage turnover meeting, reviewed PERs, and reviewed the
    that the as-built installation complied with design requirements delineated in approved
defense-in-depth status sheets to verify that status control was commensurate
    design documents. Additionally, the inspectors reviewed selected PERs to verify that
with the outage safety plan and in compliance with the applicable TS when
    plant problems were evaluated for root/apparent causes, extent of condition, and that
taking equipment out-of-service. The inspectors further toured the main control
    the developed corrective actions were adequate to ensure recurrence control of the
room and areas of the plant daily to ensure that the following key safety
    identified plant problem.
functions were maintained in accordance with the outage safety plan and TS:
  b. Findings
electrical power, decay heat removal, spent fuel cooling, inventory control,
    No findings of significance were identified.
reactivity control, and containment closure. The inspectors also observed a
1R19 Post-Maintenance Testing
tagout of the containment spray heat exchanger to verify that the equipment was
  a. Inspection Scope
appropriately configured to safely support the work or testing. To ensure that
    The inspectors reviewed the five post-maintenance tests listed below to verify that
RCS level instrumentation was properly installed and configured to give accurate
    procedures and test activities ensured system operability and functional capability. The
information, the inspectors reviewed the installation of the Mansell level  
    inspectors reviewed the licensees test procedure to verify that the procedure
18Enclosuremonitoring system. Specifically, the inspectors discussed the system withengineering, walked it down to verify that it was installed in accordance with
    adequately tested the safety function(s) that may have been affected by the
procedures and adequately protected from inadvertent damage, verified that
    maintenance activity, that the acceptance criteria in the procedure were consistent with
Mansell indication properly overlapped with pressurizer level instruments during
    information in the applicable licensing basis and/or design basis documents, and that
pressurizer draindown, verified that operators properly set level alarms to
    the procedure had been properly reviewed and approved. The inspectors also
procedurally required setpoints, and verified that the system consistently tracked  
    witnessed the test or reviewed the test data, to verify that test results adequately
while lowering RCS level to reduced inventory conditions. The inspectors also
    demonstrated restoration of the affected safety function(s). Documents reviewed are
observed operators compare the Mansell indications with locally-installed
    listed in the Attachment to this report.
ultrasonic level indicators during entry into mid-loop conditions.*Refueling Activities. The inspectors observed fuel movement at the spent fuelpool and at the refueling cavity in order to verify compliance with TS and that
    *       WO 05-782379-000, Breaker Changeout for Motor-driven Auxiliary Feedwater
each assembly was properly tracked from core offload to core reload. In order to
              (AFW) Pump 2B
verify proper licensee control of foreign material, the inspectors verified that
    *       2-SI-OPS-000-009.0, Actuation of Emergency Core Cooling Systems (ECCS)
personnel were properly checked before entering any foreign material exclusion
              and Boron Injection Flowpath Valves Via SI Signal, Revision 1
(FME) areas, reviewed FME procedures, and verified that the licensee followed
    *       WO 05-777912-001, Repack SI system Hot Leg Injection Valve, 2-FCV-63-156
the procedures. To ensure that fuel assemblies were loaded in the core
                                                                                      Enclosure
locations specified by the design, the inspectors independently reviewed the
 
recording of the licensee's final core verification.*Reduced Inventory and Mid-Loop Conditions. Prior to the outage, the inspectorsreviewed the licensee's commitments to Generic 88-17, "Loss of Decay Heat
                                              17
Removal. Before entering reduced inventory conditions the inspectors verified
    *       WO 06-780773-000, Calibrate FCV and Limit Switches on 2-FCV-074-28
that these commitments were in place, that plant configuration was in
    *       2-SI-SLT-088-156.0, Containment Integrated Leak Rate Test, Revision 2
accordance with those commitments, and that distractions from unexpected
  b. Findings
conditions or emergent work did not affect operator ability to maintain the
    No findings of significance were identified.
required reactor vessel level. While in mid-loop conditions, the inspectors
1R20 Refueling and Other Outage Activities
verified that licensee procedures for closing the containment upon a loss of
  a. Inspection Scope
decay heat removal were in effect, that operators were aware of how to
    For the Unit 2 refueling outage that began on November 27, 2006, the inspectors
implement the procedures, and that other personnel were available to close
    evaluated licensee activities to verify that the licensee considered risk in developing
containment penetrations if needed.*Heatup and Startup Activities. The inspectors toured the containment prior toreactor startup to verify that debris that could affect the performance of the
    outage schedules, followed risk reduction methods developed to control plant
containment sump had not been left in the containment. The inspectors
    configuration, developed mitigation strategies for the loss of key safety functions, and
reviewed the licensee's mode change checklists to verify that appropriate
    adhered to operating license and TS requirements that ensure defense-in-depth. The
prerequisites were met prior to changing TS modes. To verify RCS integrity and
    inspectors also walked down portions of Unit 2 not normally accessible during at-power
containment integrity, the inspectors further reviewed the licensee's RCS
    operations to verify that safety-related and risk-significant SSCs were maintained in an
leakage calculations and containment isolation valve lineups. In order to verify
    operable condition. Specifically, between November 27, 2006, and December 26, 2006,
that core operating limit parameters were consistent with core design, the
    the inspectors performed inspections and reviews of the following outage activities.
inspectors also reviewed low power physics testing results and the Core
    Documents reviewed are listed in the Attachment to this report.
Operating Limits Report.   b.FindingsNo findings of significance were identified.  
    *       Outage Plan. The inspectors reviewed the outage safety plan and contingency
19Enclosure1R22Surveillance Testing   a.Inspection ScopeFor the seven surveillance tests identified below, by witnessing testing and/or reviewingthe test data, the inspectors verified that the SSCs involved in these tests satisfied the
            plans to confirm that the licensee had appropriately considered risk, industry
requirements described in the TS surveillance requirements, the UFSAR, applicable licensee procedures, and that the tests demonstrated that the SSCs were capable of performing their intended safety functions. Documents reviewed are listed in the
            experience, and previous site-specific problems in developing and implementing
Attachment to this report. Those tests included the following:*1-SI-MIN-061-108.0, Ice Condenser Intermediate Deck Door Weekly Inspection,Revision 2*2-SI-ICC-090-106.0, Channel Calibration of Containment Building LowerCompartment Air Monitor 2-R-90-106, Revision 9****0-SI-SXV-001-859.0, Testing and Setting of Main Steam Safety Valves, Revision 9
            a plan that assured maintenance of defense-in-depth.
*2-SI-OPS-082-026.A, Loss of Offsite Power with SI - DG 2A-A Test, Revision 35
    *       Reactor Shutdown. The inspectors observed the shutdown in the control room
*0-SI-MIN-061-109.0, Ice Condenser Intermediate and Lower Inlet Doors andVent Curtains, Revision 4**2-SI-OPS-003-118.0 AFW pump and Valve Auto Actuation, Revision 18
            from the time the reactor was tripped until operators placed it on the RHR
*2-SI-SXP-003-003-202.S, Turbine Driven Auxiliary Feedwater Pump 2A-SComprehensive Performance Test, Revision 4** *This procedure included an outage ice condenser system surveillance**This procedure included inservice testing requirements
            system for decay heat removal to verify that TS cooldown restrictions were
***This procedure included a RCS leakage detection surveillance   b.FindingsNo findings of significance were identified.
            followed. The inspectors also toured the lower containment as soon as
Cornerstone: Emergency Preparedness1EP6Drill Evaluation   a.Inspection ScopeResident inspectors evaluated the conduct of a routine licensee emergency drill onOctober 3, 2006, to identify any weaknesses and deficiencies in classification,
            practicable after reactor shutdown to observe the general condition of the RCS
notification, and protective action recommendation (PARs) development activities. The
            and emergency core cooling system components and to look for indications of
inspectors observed emergency response operations in the simulated control room to
            previously unidentified leakage inside the polar crane wall.
verify that event classification and notifications were done in accordance with EPIP-1,
    *       Licensee Control of Outage Activities. On a daily basis, the inspectors attended
Emergency Plan Classification Matrix, Revision 38. The inspectors also attended the
            the licensee outage turnover meeting, reviewed PERs, and reviewed the
licensee critique of the drill to compare any inspector-observed weakness with those
            defense-in-depth status sheets to verify that status control was commensurate
identified by the licensee in order to verify whether the licensee was properly identifying
            with the outage safety plan and in compliance with the applicable TS when
failures. Documents reviewed are listed in the Attachment to this report.  
            taking equipment out-of-service. The inspectors further toured the main control
20Enclosure   b.FindingsNo findings of significance were identified.2.RADIATION SAFETYCornerstone: Occupational Radiation Safety (OS)2OS1Access Control To Radiologically Significant Areas    a.Inspection Scope
            room and areas of the plant daily to ensure that the following key safety
Access Control Licensee program activities for monitoring workers and controllingaccess to radiologically significant areas and tasks were inspected. The inspector
            functions were maintained in accordance with the outage safety plan and TS:
evaluated procedural guidance; directly observed implementation of administrative and
            electrical power, decay heat removal, spent fuel cooling, inventory control,
established physical controls; assessed worker exposures to radiation and radioactive  
            reactivity control, and containment closure. The inspectors also observed a
material; and appraised radiation worker and technician knowledge of, and proficiencyin, the implementation of Radiation Protection (RP) program activities.During the inspection, radiological controls for ongoing refueling activities for Unit 2 wereobserved and discussed. Reviewed tasks included steam generator non-destructive
            tagout of the containment spray heat exchanger to verify that the equipment was
testing, containment sump modifications, and refueling activities. In addition, licensee
            appropriately configured to safely support the work or testing. To ensure that
controls for selected tasks scheduled and on-going during the current refueling outage
            RCS level instrumentation was properly installed and configured to give accurate
were assessed. The evaluations included, as applicable, Radiation Work Permit (RWP)
            information, the inspectors reviewed the installation of the Mansell level
details; use and placement of dosimetry and air sampling equipment; electronic
                                                                                        Enclosure
dosimeter set-points, and monitoring and assessment of worker dose from direct
 
radiation and airborne radioactivity source terms. Effectiveness of established controls
                                            18
was assessed against area radiation and contamination survey results, and
          monitoring system. Specifically, the inspectors discussed the system with
occupational doses received. Physical and administrative controls and their
          engineering, walked it down to verify that it was installed in accordance with
implementation for locked high radiation areas (LHRAs) and very high radiation areaswere evaluated through discussions with cognizant licensee representatives, direct field
          procedures and adequately protected from inadvertent damage, verified that
observations, and record reviews.Occupational workers' adherence to selected radiation work permits (RWPs) and HealthPhysics Technician proficiency in providing job coverage were evaluated through direct
          Mansell indication properly overlapped with pressurizer level instruments during
observations of staff performance during job coverage and routine surveillance
          pressurizer draindown, verified that operators properly set level alarms to
activities, review of selected exposure records, and interviews with cognizant licensee
          procedurally required setpoints, and verified that the system consistently tracked
staff. Radiological postings and physical controls for access to designated high
          while lowering RCS level to reduced inventory conditions. The inspectors also
radiation (HRA) and LHRA locations within the Unit 2 Containment, Auxiliary Building,
          observed operators compare the Mansell indications with locally-installed
and Refuel Floor areas were evaluated during facility tours. In addition, the inspectors
          ultrasonic level indicators during entry into mid-loop conditions.
independently measured radiation dose rates and evaluated established posting and
  *     Refueling Activities. The inspectors observed fuel movement at the spent fuel
access controls for selected Auxiliary Building locations. Occupational exposures
          pool and at the refueling cavity in order to verify compliance with TS and that
associated with direct radiation and potential radioactive material intakes for were
          each assembly was properly tracked from core offload to core reload. In order to
reviewed and discussed with cognizant licensee representatives.RP program activities were evaluated against 10 CFR 19.12; 10 CFR 20, Subparts B, C,F, G, H, and J; UFSAR details in Section 12, RP; TSs Section 6.11, High Radiation
          verify proper licensee control of foreign material, the inspectors verified that
Area; and approved licensee procedures. Licensee procedures, guidance documents,  
          personnel were properly checked before entering any foreign material exclusion
21Enclosurerecords, and data reviewed within this inspection area are listed in Section 2OS1 of theAttachment to this report.Problem Identification and Resolution Licensee Corrective Action Program documentsassociated with access control to radiologically significant areas were reviewed and
          (FME) areas, reviewed FME procedures, and verified that the licensee followed
assessed. The inspectors evaluated the licensee's ability to identify, characterize,
          the procedures. To ensure that fuel assemblies were loaded in the core
prioritize, and resolve the identified issues in accordance with Standard Programs and
          locations specified by the design, the inspectors independently reviewed the
Processes procedure SPP-3.1, Corrective Action Program. Licensee self-assessments
          recording of the licensees final core verification.
and PER documents related to access control that were reviewed and evaluated in
  *     Reduced Inventory and Mid-Loop Conditions. Prior to the outage, the inspectors
detail during inspection of this program area are identified in Section 2OS1 of the
          reviewed the licensees commitments to Generic 88-17, Loss of Decay Heat
Attachment to this report.The inspector completed 21 of the required 21 samples for Inspection Procedure (IP)71121.01. All samples have now been completed for this IP.    b.FindingsNo findings of significance were identified.4.OTHER ACTIVITIES
          Removal. Before entering reduced inventory conditions the inspectors verified
4OA2Identification and Resolution of Problems.1Daily Review
          that these commitments were in place, that plant configuration was in
  As required by Inspection Procedure 71152, Identification and Resolution of Problems,and in order to help identify repetitive equipment failures or specific human performance
          accordance with those commitments, and that distractions from unexpected
issues for follow-up, the inspectors performed a daily screening of items entered into the
          conditions or emergent work did not affect operator ability to maintain the
licensee's corrective action program. This was accomplished by reviewing the
          required reactor vessel level. While in mid-loop conditions, the inspectors
description of each new PER and attending daily management review committee
          verified that licensee procedures for closing the containment upon a loss of
meetings..2Semi-Annual Trend Review
          decay heat removal were in effect, that operators were aware of how to
    a.Inspection ScopeAs required by Inspection Procedure 71152, the inspectors performed a review of thelicensee's corrective action program and associated documents to identify trends that
          implement the procedures, and that other personnel were available to close
could indicate the existence of a more significant safety issue. The inspectors' review
          containment penetrations if needed.
was focused on procedure quality and compliance issues, but also included licensee
  *     Heatup and Startup Activities. The inspectors toured the containment prior to
trending efforts and licensee human performance results. The inspectors' review
          reactor startup to verify that debris that could affect the performance of the
nominally considered the six-month period of July 2006 through December 2006,
          containment sump had not been left in the containment. The inspectors
although some examples expanded beyond those dates when the scope of the trend
          reviewed the licensees mode change checklists to verify that appropriate
warranted. Specifically, the inspectors consolidated the results of daily inspector screeningdiscussed in Section 4OA2.1 into a log, reviewed the log, and compared it to licensee
          prerequisites were met prior to changing TS modes. To verify RCS integrity and
integrated quarterly trend reports for the period from July 2006 through September 2006  
          containment integrity, the inspectors further reviewed the licensees RCS
22Enclosurein order to determine the existence of any adverse trends that the licensee may nothave previously identified.    b.Assessment and ObservationsThe inspectors identified issues with procedure quality and compliance over the periodof assessment. Noteworthy examples of deficient procedure quality or compliance
          leakage calculations and containment isolation valve lineups. In order to verify
were:*PER 114003, Incorrect Procedure Revision used on 6.9kV Shutdown Board relay
          that core operating limit parameters were consistent with core design, the
testing*PER 115490, Inability to manually operate Appendix R valves within the requiredtime.*PER 115539, Emergency Gas Treatment System procedure cloning resulting infailure of Unit 2 Phase A testing requirements.*PER 115534, Loss of RCS inventory during Unit 2 refueling outage Mansellalignment.*PER 117008, Missed firewatch through plant areas with disabled fire detection.No findings of significance were identified. In general, the licensee had identified trendsand appropriately communicated them to plant senior management. The inspectors
          inspectors also reviewed low power physics testing results and the Core
evaluated the licensee trending methodology and observed that the licensee had
          Operating Limits Report.
performed a summary review of issues which were inputs to the plant Human
b. Findings
Performance Index. The licensee reviewed cause codes, involved organizations, key
  No findings of significance were identified.
words, and system links to identify potential trends in the data. The inspectors
                                                                                    Enclosure
compared the licensee process results with the results of the inspectors' daily
 
screenings and did not identify any significant discrepancies or potential trends that the
                                                19
licensee had failed to identify. The specifics surrounding PER 115490, regarding the
1R22 Surveillance Testing
inability to manually operate Appendix R valves within the required time, are further
  a. Inspection Scope
addressed in Section 1R15, Operability Evaluations..3Annual Sample Review of Problems with Plant Venting Operations    a.Inspection ScopeThe inspectors reviewed licensee actions to resolve issues surrounding plant ventingoperations. This review began as a look at how the licensee addressed problems
    For the seven surveillance tests identified below, by witnessing testing and/or reviewing
associated with two potentially significant events that had occurred during the venting of
    the test data, the inspectors verified that the SSCs involved in these tests satisfied the
plant systems. These events are common to nuclear plant operations and often are
    requirements described in the TS surveillance requirements, the UFSAR, applicable
required in restoration of a system after it has been removed from service or opened for
    licensee procedures, and that the tests demonstrated that the SSCs were capable of
maintenance. PER 92485 was written on November 21, 2005, and identified that
    performing their intended safety functions. Documents reviewed are listed in the
operators had discovered the collapse of the "A" Chemical Volume Control System
    Attachment to this report. Those tests included the following:
(CVCS) Holdup Tank (HUT) due to the lack of an adequate vent path during drain down.  
    *       1-SI-MIN-061-108.0, Ice Condenser Intermediate Deck Door Weekly Inspection,
The licensee subsequently suspended use of the "A" CVCS HUT, performed a root
              Revision 2
cause analysis, and implemented corrective actions to prevent a recurrence of this
    *       2-SI-ICC-090-106.0, Channel Calibration of Containment Building Lower
activity. The inspectors reviewed the completion of required actions items spawned
              Compartment Air Monitor 2-R-90-106, Revision 9***
from this event for timeliness, accuracy and adequacy. PER 102591 was written on
    *       0-SI-SXV-001-859.0, Testing and Setting of Main Steam Safety Valves, Revision 9
May 7, 2006, to address an event during drain down of the RCS to midloop conditions.  
    *       2-SI-OPS-082-026.A, Loss of Offsite Power with SI - DG 2A-A Test, Revision 35
While making preparations for vacuum refill of the RCS, the evolution had to be  
    *       0-SI-MIN-061-109.0, Ice Condenser Intermediate and Lower Inlet Doors and
23Enclosuresuspended when it was identified that a required reactor vessel head vent path was notproperly aligned. The licensee immediately vented the RCS and verified that the RCS
              Vent Curtains, Revision 4*
was not under vacuum conditions based on no observed change in RCS level indication
    *       2-SI-OPS-003-118.0 AFW pump and Valve Auto Actuation, Revision 18
when the head vent was opened. The licensee declared that the apparent cause of the
    *       2-SI-SXP-003-003-202.S, Turbine Driven Auxiliary Feedwater Pump 2A-S
event was due to failure to follow procedure, inadequate procedural guidance, and
              Comprehensive Performance Test, Revision 4**
inadequate scheduling. The event associated with PER 102591 was dispositioned as a
    *This procedure included an outage ice condenser system surveillance
licensee-identified violation in Inspection Report 05000327, 328/2006003. The
    **This procedure included inservice testing requirements
inspectors reviewed the PER action items for adequacy and the associated procedures
    ***This procedure included a RCS leakage detection surveillance
to ensure changes were implemented to preclude repetition of this event. The
  b. Findings
inspectors utilized these examples during the inspection period to observe similar
    No findings of significance were identified.
activities that had the potential to degrade in risk significant systems. The inspectors
    Cornerstone: Emergency Preparedness
were able to observe RCS drain down and refill activities during the Unit 2 Cycle 14
1EP6 Drill Evaluation
refueling outage, as well as, the venting operations of support systems during
  a. Inspection Scope
restoration to their normal mode of operation.     b.Findings and ObservationsNo findings of significance were identified. The inspectors noted that the licenseeappeared to have an adequate sensitivity to operational experience, procedural
    Resident inspectors evaluated the conduct of a routine licensee emergency drill on
guidance, scheduling conflicts, and foreign material exclusion. The licensee was
    October 3, 2006, to identify any weaknesses and deficiencies in classification,
successful in properly performing the necessary venting activities associated with the  
    notification, and protective action recommendation (PARs) development activities. The
multiple system drain and refill operations accompanying Unit 2 refueling outage
    inspectors observed emergency response operations in the simulated control room to
maintenance.4OA5Other Activities.1Review of the Operation of an Independent Spent Fuel Storage Installation (ISFSI)(60855.1)    a.Inspection ScopeThe inspectors reviewed ISFSI document control practices to verify that changes to therequired ISFSI procedures and equipment were performed in accordance with
    verify that event classification and notifications were done in accordance with EPIP-1,
guidelines established in licensee procedures and 10 CFR 72.48. Documents reviewed
    Emergency Plan Classification Matrix, Revision 38. The inspectors also attended the
are listed in the Attachment to this report.    b.FindingsNo findings of significance were identified..2(Open) NRC Temporary Instruction 2515/150, Rev. 2, Reactor Pressure Vessel Headand Vessel Head Penetration Nozzles (NRC Order EA-03-009) - Unit 2    a.Inspection Scope
    licensee critique of the drill to compare any inspector-observed weakness with those
From December 4 - 8, 2006, the inspectors reviewed the licensee's activities associatedwith the NDE of the reactor pressure vessel head (RPVH) penetration nozzles, the bare
    identified by the licensee in order to verify whether the licensee was properly identifying
metal visual examination of the top surface of the RPVH, and the visual examination toidentify potential boric acid leaks from pressure-retaining components above the RPVH.  
    failures. Documents reviewed are listed in the Attachment to this report.
24EnclosureThese activities were performed in response to NRC Bulletins 2001-01, 2002-01, 2002-02, and the first revision of NRC Order EA-03-009 Modifying Licenses dated February
                                                                                      Enclosure
20, 2004 (hereafter referred to as the NRC Order). The inspectors' review of the NDE of RPVH penetration nozzles included independentobservation and evaluation of ultrasonic testing (UT) examinations (for both data
 
acquisition and analysis), review of NDE procedures, personnel qualifications and
                                              20
training, and NDE equipment certifications. The inspectors also held interviews with
   b. Findings
contractor representatives (Areva) and other licensee personnel involved with the RPVH
      No findings of significance were identified.
examination. The activities were reviewed to verify licensee compliance with the NRC
2.   RADIATION SAFETY
Order and to gather information to help the NRC staff identify possible further regulatory
      Cornerstone: Occupational Radiation Safety (OS)
positions and generic communications.The inspectors reviewed a sample of the results from the volumetric UT examinations ofRPVH penetration nozzles. Specifically, the inspectors reviewed or observed the
2OS1 Access Control To Radiologically Significant Areas
following:*Observed in-process UT data acquisition scanning of RPVH penetration nozzles57 and 52 (both with thermal sleeves)*Reviewed the UT electronic data with the Level III analyst for RPVH nozzles 4,36, 43, 50, 56, 61, 69, 77, 126 and the calibration block (this included nozzles
   a. Inspection Scope
both with and without thermal sleeves)*Reviewed the results of the UT examination performed to assess for leakage intothe annulus (interference fit zone) between the RPVH penetration nozzle and the
      Access Control Licensee program activities for monitoring workers and controlling
RPVH low-alloy steel for all penetration numbers listed in the previous bullet *Reviewed the procedures and results for the visual exam performed to identifypotential boric acid leaks from pressure-retaining components above the RPVH*Reviewed the RPVH susceptibility ranking and calculation of effectivedegradation years (EDY), including the basis for the RPVH temperature used in
      access to radiologically significant areas and tasks were inspected. The inspector
the calculation b. Observations and FindingsIn accordance with the requirements of TI 2515/150, the inspectors evaluated andanswered the following questions:1) Were the examinations performed by qualified and knowledgeable personnel?
      evaluated procedural guidance; directly observed implementation of administrative and
Yes. All personnel involved with the RPVH inspections were appropriately qualified inaccordance with the ASME Code, and most far exceeded the minimum requirements for
      established physical controls; assessed worker exposures to radiation and radioactive
experience and training hours. The contractor (Areva) personnel responsible for
      material; and appraised radiation worker and technician knowledge of, and proficiency
equipment manipulation, data acquisition, and data analysis frequently perform these
      in, the implementation of Radiation Protection (RP) program activities.
types of inspections nationwide.  
      During the inspection, radiological controls for ongoing refueling activities for Unit 2 were
25Enclosure2) Were the examinations performed in accordance with demonstratedprocedures?Yes. The Sequoyah Unit 2 RPVH has 57 control rod drive mechanism (CRDM) nozzleswith thermal sleeves, 13 with open housings (including 5 instrument column nozzles), 8
      observed and discussed. Reviewed tasks included steam generator non-destructive
      testing, containment sump modifications, and refueling activities. In addition, licensee
      controls for selected tasks scheduled and on-going during the current refueling outage
      were assessed. The evaluations included, as applicable, Radiation Work Permit (RWP)
      details; use and placement of dosimetry and air sampling equipment; electronic
      dosimeter set-points, and monitoring and assessment of worker dose from direct
      radiation and airborne radioactivity source terms. Effectiveness of established controls
      was assessed against area radiation and contamination survey results, and
      occupational doses received. Physical and administrative controls and their
      implementation for locked high radiation areas (LHRAs) and very high radiation areas
      were evaluated through discussions with cognizant licensee representatives, direct field
      observations, and record reviews.
      Occupational workers adherence to selected radiation work permits (RWPs) and Health
      Physics Technician proficiency in providing job coverage were evaluated through direct
      observations of staff performance during job coverage and routine surveillance
      activities, review of selected exposure records, and interviews with cognizant licensee
      staff. Radiological postings and physical controls for access to designated high
      radiation (HRA) and LHRA locations within the Unit 2 Containment, Auxiliary Building,
      and Refuel Floor areas were evaluated during facility tours. In addition, the inspectors
      independently measured radiation dose rates and evaluated established posting and
      access controls for selected Auxiliary Building locations. Occupational exposures
      associated with direct radiation and potential radioactive material intakes for were
      reviewed and discussed with cognizant licensee representatives.
      RP program activities were evaluated against 10 CFR 19.12; 10 CFR 20, Subparts B, C,
      F, G, H, and J; UFSAR details in Section 12, RP; TSs Section 6.11, High Radiation
      Area; and approved licensee procedures. Licensee procedures, guidance documents,
                                                                                        Enclosure
 
                                                21
      records, and data reviewed within this inspection area are listed in Section 2OS1 of the
      Attachment to this report.
      Problem Identification and Resolution Licensee Corrective Action Program documents
      associated with access control to radiologically significant areas were reviewed and
      assessed. The inspectors evaluated the licensees ability to identify, characterize,
      prioritize, and resolve the identified issues in accordance with Standard Programs and
      Processes procedure SPP-3.1, Corrective Action Program. Licensee self-assessments
      and PER documents related to access control that were reviewed and evaluated in
      detail during inspection of this program area are identified in Section 2OS1 of the
      Attachment to this report.
      The inspector completed 21 of the required 21 samples for Inspection Procedure (IP)
      71121.01. All samples have now been completed for this IP.
   b. Findings
      No findings of significance were identified.
4.   OTHER ACTIVITIES
4OA2 Identification and Resolution of Problems
.1    Daily Review
      As required by Inspection Procedure 71152, Identification and Resolution of Problems,
      and in order to help identify repetitive equipment failures or specific human performance
      issues for follow-up, the inspectors performed a daily screening of items entered into the
      licensees corrective action program. This was accomplished by reviewing the
      description of each new PER and attending daily management review committee
      meetings.
.2    Semi-Annual Trend Review
  a. Inspection Scope
      As required by Inspection Procedure 71152, the inspectors performed a review of the
      licensees corrective action program and associated documents to identify trends that
      could indicate the existence of a more significant safety issue. The inspectors review
      was focused on procedure quality and compliance issues, but also included licensee
      trending efforts and licensee human performance results. The inspectors review
      nominally considered the six-month period of July 2006 through December 2006,
      although some examples expanded beyond those dates when the scope of the trend
      warranted.
      Specifically, the inspectors consolidated the results of daily inspector screening
      discussed in Section 4OA2.1 into a log, reviewed the log, and compared it to licensee
      integrated quarterly trend reports for the period from July 2006 through September 2006
                                                                                        Enclosure
 
                                                22
      in order to determine the existence of any adverse trends that the licensee may not
      have previously identified.
   b. Assessment and Observations
      The inspectors identified issues with procedure quality and compliance over the period
      of assessment. Noteworthy examples of deficient procedure quality or compliance
      were:
      *       PER 114003, Incorrect Procedure Revision used on 6.9kV Shutdown Board relay
              testing
      *       PER 115490, Inability to manually operate Appendix R valves within the required
              time.
      *       PER 115539, Emergency Gas Treatment System procedure cloning resulting in
              failure of Unit 2 Phase A testing requirements.
      *       PER 115534, Loss of RCS inventory during Unit 2 refueling outage Mansell
              alignment.
      *       PER 117008, Missed firewatch through plant areas with disabled fire detection.
      No findings of significance were identified. In general, the licensee had identified trends
      and appropriately communicated them to plant senior management. The inspectors
      evaluated the licensee trending methodology and observed that the licensee had
      performed a summary review of issues which were inputs to the plant Human
      Performance Index. The licensee reviewed cause codes, involved organizations, key
      words, and system links to identify potential trends in the data. The inspectors
      compared the licensee process results with the results of the inspectors daily
      screenings and did not identify any significant discrepancies or potential trends that the
      licensee had failed to identify. The specifics surrounding PER 115490, regarding the
      inability to manually operate Appendix R valves within the required time, are further
      addressed in Section 1R15, Operability Evaluations.
.3    Annual Sample Review of Problems with Plant Venting Operations
   a. Inspection Scope
      The inspectors reviewed licensee actions to resolve issues surrounding plant venting
      operations. This review began as a look at how the licensee addressed problems
      associated with two potentially significant events that had occurred during the venting of
      plant systems. These events are common to nuclear plant operations and often are
      required in restoration of a system after it has been removed from service or opened for
      maintenance. PER 92485 was written on November 21, 2005, and identified that
      operators had discovered the collapse of the A Chemical Volume Control System
      (CVCS) Holdup Tank (HUT) due to the lack of an adequate vent path during drain down.
      The licensee subsequently suspended use of the A CVCS HUT, performed a root
      cause analysis, and implemented corrective actions to prevent a recurrence of this
      activity. The inspectors reviewed the completion of required actions items spawned
      from this event for timeliness, accuracy and adequacy. PER 102591 was written on
      May 7, 2006, to address an event during drain down of the RCS to midloop conditions.
      While making preparations for vacuum refill of the RCS, the evolution had to be
                                                                                        Enclosure
 
                                                23
      suspended when it was identified that a required reactor vessel head vent path was not
      properly aligned. The licensee immediately vented the RCS and verified that the RCS
      was not under vacuum conditions based on no observed change in RCS level indication
      when the head vent was opened. The licensee declared that the apparent cause of the
      event was due to failure to follow procedure, inadequate procedural guidance, and
      inadequate scheduling. The event associated with PER 102591 was dispositioned as a
      licensee-identified violation in Inspection Report 05000327, 328/2006003. The
      inspectors reviewed the PER action items for adequacy and the associated procedures
      to ensure changes were implemented to preclude repetition of this event. The
      inspectors utilized these examples during the inspection period to observe similar
      activities that had the potential to degrade in risk significant systems. The inspectors
      were able to observe RCS drain down and refill activities during the Unit 2 Cycle 14
      refueling outage, as well as, the venting operations of support systems during
      restoration to their normal mode of operation.
  b. Findings and Observations
      No findings of significance were identified. The inspectors noted that the licensee
      appeared to have an adequate sensitivity to operational experience, procedural
      guidance, scheduling conflicts, and foreign material exclusion. The licensee was
      successful in properly performing the necessary venting activities associated with the
      multiple system drain and refill operations accompanying Unit 2 refueling outage
      maintenance.
4OA5 Other Activities
.1    Review of the Operation of an Independent Spent Fuel Storage Installation (ISFSI)
      (60855.1)
   a. Inspection Scope
      The inspectors reviewed ISFSI document control practices to verify that changes to the
      required ISFSI procedures and equipment were performed in accordance with
      guidelines established in licensee procedures and 10 CFR 72.48. Documents reviewed
      are listed in the Attachment to this report.
   b. Findings
      No findings of significance were identified.
.2   (Open) NRC Temporary Instruction 2515/150, Rev. 2, Reactor Pressure Vessel Head
      and Vessel Head Penetration Nozzles (NRC Order EA-03-009) - Unit 2
   a. Inspection Scope
      From December 4 - 8, 2006, the inspectors reviewed the licensees activities associated
      with the NDE of the reactor pressure vessel head (RPVH) penetration nozzles, the bare
      metal visual examination of the top surface of the RPVH, and the visual examination to
      identify potential boric acid leaks from pressure-retaining components above the RPVH.
                                                                                        Enclosure
 
                                            24
  These activities were performed in response to NRC Bulletins 2001-01, 2002-01, 2002-
  02, and the first revision of NRC Order EA-03-009 Modifying Licenses dated February
  20, 2004 (hereafter referred to as the NRC Order).
  The inspectors review of the NDE of RPVH penetration nozzles included independent
  observation and evaluation of ultrasonic testing (UT) examinations (for both data
  acquisition and analysis), review of NDE procedures, personnel qualifications and
  training, and NDE equipment certifications. The inspectors also held interviews with
  contractor representatives (Areva) and other licensee personnel involved with the RPVH
  examination. The activities were reviewed to verify licensee compliance with the NRC
  Order and to gather information to help the NRC staff identify possible further regulatory
  positions and generic communications.
  The inspectors reviewed a sample of the results from the volumetric UT examinations of
  RPVH penetration nozzles. Specifically, the inspectors reviewed or observed the
  following:
  *       Observed in-process UT data acquisition scanning of RPVH penetration nozzles
          57 and 52 (both with thermal sleeves)
  *       Reviewed the UT electronic data with the Level III analyst for RPVH nozzles 4,
          36, 43, 50, 56, 61, 69, 77, 126 and the calibration block (this included nozzles
          both with and without thermal sleeves)
  *       Reviewed the results of the UT examination performed to assess for leakage into
          the annulus (interference fit zone) between the RPVH penetration nozzle and the
          RPVH low-alloy steel for all penetration numbers listed in the previous bullet
  *       Reviewed the procedures and results for the visual exam performed to identify
          potential boric acid leaks from pressure-retaining components above the RPVH
  *       Reviewed the RPVH susceptibility ranking and calculation of effective
          degradation years (EDY), including the basis for the RPVH temperature used in
          the calculation
b. Observations and Findings
  In accordance with the requirements of TI 2515/150, the inspectors evaluated and
  answered the following questions:
  1)     Were the examinations performed by qualified and knowledgeable personnel?
  Yes. All personnel involved with the RPVH inspections were appropriately qualified in
  accordance with the ASME Code, and most far exceeded the minimum requirements for
  experience and training hours. The contractor (Areva) personnel responsible for
  equipment manipulation, data acquisition, and data analysis frequently perform these
  types of inspections nationwide.
                                                                                    Enclosure
 
                                        25
2)       Were the examinations performed in accordance with demonstrated
        procedures?
Yes. The Sequoyah Unit 2 RPVH has 57 control rod drive mechanism (CRDM) nozzles
with thermal sleeves, 13 with open housings (including 5 instrument column nozzles), 8
with part lengths, 4 upper head injection (UHI) nozzles, and 1 vent line nozzle, for a total
with part lengths, 4 upper head injection (UHI) nozzles, and 1 vent line nozzle, for a total
of 83 nozzles. All nozzles were subject to remote automated UT examination using one
of 83 nozzles. All nozzles were subject to remote automated UT examination using one
of two types of probes. The blade probe was used for sleeved penetrations and the
of two types of probes. The blade probe was used for sleeved penetrations and the
open housing CRDMs using a dummy sleeve. The rotating probe was used for the
open housing CRDMs using a dummy sleeve. The rotating probe was used for the
other open housing penetrations (UHI and instrument columns). A liquid penetrant
other open housing penetrations (UHI and instrument columns). A liquid penetrant
exam on the surface of the J-groove weld of the vent line was also performed to satisfy
exam on the surface of the J-groove weld of the vent line was also performed to satisfy
the NRC Order. Procedures 54-ISI-603-002 (UT with thermal sleeves), 54-ISI-604-001 (UT of openhousings), 54-ISI-605-02 (UT of vent line), and 54-ISI-240-44 (liquid penetrant) were
the NRC Order.
implemented to complete the exams described above. Further, the inspectors verified
Procedures 54-ISI-603-002 (UT with thermal sleeves), 54-ISI-604-001 (UT of open
housings), 54-ISI-605-02 (UT of vent line), and 54-ISI-240-44 (liquid penetrant) were
implemented to complete the exams described above. Further, the inspectors verified
that the 54-ISI-603-002 and 54-ISI-604-001 procedures were used during the Areva
that the 54-ISI-603-002 and 54-ISI-604-001 procedures were used during the Areva
demonstration to EPRI's Materials Reliability Program (MRP) to show flaw detection
demonstration to EPRIs Materials Reliability Program (MRP) to show flaw detection
capability in RPVH penetrations. By letter dated October 3, 2006, from Jack Spanner of
capability in RPVH penetrations. By letter dated October 3, 2006, from Jack Spanner of
EPRI to Joel Whitaker of TVA (the licensee), EPRI stated that Areva's demonstration of
EPRI to Joel Whitaker of TVA (the licensee), EPRI stated that Arevas demonstration of
flaw detection techniques could reliably detect flaws in CRDM penetrations.3) Was the examination able to identify, disposition, and resolve deficiencies?
flaw detection techniques could reliably detect flaws in CRDM penetrations.
Yes. All indications of cracks or interference fit zone leakage are required to bereported for further examination and disposition. Based on observation of the
3)       Was the examination able to identify, disposition, and resolve deficiencies?
Yes. All indications of cracks or interference fit zone leakage are required to be
reported for further examination and disposition. Based on observation of the
examination process, the inspectors considered deficiencies would be appropriately
examination process, the inspectors considered deficiencies would be appropriately
identified, dispositioned, and resolved. UT indications associated with the geometry of
identified, dispositioned, and resolved. UT indications associated with the geometry of
the examined volume were identified in several penetration tubes. None of the
the examined volume were identified in several penetration tubes. None of the
indications exhibited crack-like characteristics and were appropriately dispositioned in
indications exhibited crack-like characteristics and were appropriately dispositioned in
accordance with procedures.4) Was the examination capable of identifying the primary water stress corrosioncracking (PWSCC) and/or RPVH corrosion phenomena described in the NRC
accordance with procedures.
Order?Yes. The NDE techniques employed for the examination of RPVH nozzles had beenpreviously demonstrated under the EPRI MRP/Inspection Demonstration Program as
4)       Was the examination capable of identifying the primary water stress corrosion
        cracking (PWSCC) and/or RPVH corrosion phenomena described in the NRC
        Order?
Yes. The NDE techniques employed for the examination of RPVH nozzles had been
previously demonstrated under the EPRI MRP/Inspection Demonstration Program as
capable of detecting PWSCC-type manufactured cracks as well as cracks from actual
capable of detecting PWSCC-type manufactured cracks as well as cracks from actual
samples from another site. Based on the demonstration, observation of in-process
samples from another site. Based on the demonstration, observation of in-process
examinations, and review of NDE data, the inspectors determined that the licensee was
examinations, and review of NDE data, the inspectors determined that the licensee was
capable of identifying PWSCC and/or corrosion as required by the NRC Order. 5) What was the physical condition of the RPVH (e.g. debris, insulation, dirt, boronfrom other sources, physical layout, viewing obstructions)?The licensee performed a 100% bare metal visual (BMV) inspection of the top of theRPVH, including 360 around each penetration using a remote visual robotic crawler forareas inside the lead shielding and underneath the raised insulation package. The  
capable of identifying PWSCC and/or corrosion as required by the NRC Order.
26Enclosuresurface sloping down from the shielding to the flange was visually inspected directly by aLevel III VT-2 examiner. The inspectors independently reviewed portions of the remoteinspection video which revealed no insulation, dirt, or other general debris that caused
5)       What was the physical condition of the RPVH (e.g. debris, insulation, dirt, boron
viewing obstructions in the areas of interest. Some small, loose particles of debris were
        from other sources, physical layout, viewing obstructions)?
easily cleared from the surface with a low-pressure air stream mounted on the remote  
The licensee performed a 100% bare metal visual (BMV) inspection of the top of the
crawler. The inspectors determined that the physical condition of the head was
RPVH, including 360E around each penetration using a remote visual robotic crawler for
adequate to meet the inspection requirements mandated by the NRC Order.6) Could small boron deposits, as described in NRC Bulletin 2001-01, be identifiedand characterized?Yes. The BMV examination was determined by the inspectors to be capable ofidentifying and characterizing small boron deposits as described in NRC Bulletin 2001-
areas inside the lead shielding and underneath the raised insulation package. The
01. The remote exam was VT-2 qualified and able to resolve, at a minimum, the 0.105-
                                                                                  Enclosure
inch characters on an ASME IWA-2210-1 Visual Illumination Card.7) What material deficiencies (i.e., cracks, corrosion, etc.) were identified thatrequired repair?There were no identified examples of RPVH penetration cracks, leakage, materialdeficiencies, head corrosion, or other flaws that required repair. As discussed
 
                                          26
surface sloping down from the shielding to the flange was visually inspected directly by a
Level III VT-2 examiner. The inspectors independently reviewed portions of the remote
inspection video which revealed no insulation, dirt, or other general debris that caused
viewing obstructions in the areas of interest. Some small, loose particles of debris were
easily cleared from the surface with a low-pressure air stream mounted on the remote
crawler. The inspectors determined that the physical condition of the head was
adequate to meet the inspection requirements mandated by the NRC Order.
6)     Could small boron deposits, as described in NRC Bulletin 2001-01, be identified
        and characterized?
Yes. The BMV examination was determined by the inspectors to be capable of
identifying and characterizing small boron deposits as described in NRC Bulletin 2001-
01. The remote exam was VT-2 qualified and able to resolve, at a minimum, the 0.105-
inch characters on an ASME IWA-2210-1 Visual Illumination Card.
7)     What material deficiencies (i.e., cracks, corrosion, etc.) were identified that
        required repair?
There were no identified examples of RPVH penetration cracks, leakage, material
deficiencies, head corrosion, or other flaws that required repair. As discussed
previously, there were some UT indications at J-groove welds that were dispositioned as
previously, there were some UT indications at J-groove welds that were dispositioned as
metallurgical/geometric indications (not service related). One metallurgical indication on
metallurgical/geometric indications (not service related). One metallurgical indication on
tube 56 actually extended below the J-groove weld, and the inspector verified that
tube 56 actually extended below the J-groove weld, and the inspector verified that
adequate coverage below this metallurgical indication was obtained. These indications
adequate coverage below this metallurgical indication was obtained. These indications
were likely due to weld repairs performed during initial RPVH fabrication.8) What, if any, impediments to effective examinations, for each of the appliedmethods, were identified (e.g., centering rings, insulation, thermal sleeves,
were likely due to weld repairs performed during initial RPVH fabrication.
instrumentation, nozzle distortion)?The penetration nozzles with thermal sleeves and centering pads did not impedeeffective examination. Concerning examination coverage, the NRC Order requires that
8)     What, if any, impediments to effective examinations, for each of the applied
each tube's volume is inspected from a minimum of 2 inches above the highest point of
        methods, were identified (e.g., centering rings, insulation, thermal sleeves,
        instrumentation, nozzle distortion)?
The penetration nozzles with thermal sleeves and centering pads did not impede
effective examination. Concerning examination coverage, the NRC Order requires that
each tubes volume is inspected from a minimum of 2 inches above the highest point of
the J-groove weld to 2 inches below the lowest point of the J-groove weld, or 1 inch with
the J-groove weld to 2 inches below the lowest point of the J-groove weld, or 1 inch with
a stress analysis. The licensee had performed a stress analysis and the inspectors
a stress analysis. The licensee had performed a stress analysis and the inspectors
verified that the minimum examination coverages required by the NRC Order were met. 9) What was the basis for the temperature used in the susceptibility rankingcalculation? NRC Order EA-03-009 requires that licensees calculate the EDY of the RPVH todetermine its susceptibility category, which subsequently determines the scope and
verified that the minimum examination coverages required by the NRC Order were met.
frequency of required RPVH examinations. The operating temperature of the RPVH is
9)     What was the basis for the temperature used in the susceptibility ranking
an input to this calculation. Therefore, an incorrect temperature input could result in
        calculation?
placing the RPVH in an incorrect susceptibility category. The licensee uses the cold leg
NRC Order EA-03-009 requires that licensees calculate the EDY of the RPVH to
temperature in this calculation.
determine its susceptibility category, which subsequently determines the scope and
27EnclosureIn Supplement No. 1 to the NRC's Safety Evaluation Report (SER) dated February1980, the NRC concluded that scale model tests provided reasonable assurance that
frequency of required RPVH examinations. The operating temperature of the RPVH is
the upper head would operate at the cold leg temperature. However, the NRC staff also
an input to this calculation. Therefore, an incorrect temperature input could result in
required that plant data be acquired to confirm the head temperature. This data was
placing the RPVH in an incorrect susceptibility category. The licensee uses the cold leg
acquired for Unit 1 to satisfy both units because Unit 2 is considered a sister plant. The
temperature in this calculation.
inspectors reviewed this data which confirmed that the head operated at approximately
                                                                                  Enclosure
cold leg temperature with some minor thermocouple variations. In addition, both units
 
underwent a modification since this testing to increase bypass flow to the head from 4%
                                                27
to about 7%. This gives further assurance that the RPVH operates at cold leg
      In Supplement No. 1 to the NRCs Safety Evaluation Report (SER) dated February
temperature. For these reasons, the inspectors concluded that the licensee had an
      1980, the NRC concluded that scale model tests provided reasonable assurance that
adequate basis for their temperature input to the susceptibility ranking calculation, which
      the upper head would operate at the cold leg temperature. However, the NRC staff also
results in Unit 2 being placed in the Low category.10) During non-visual examinations, was the disposition of indications consistent withthe NRC flaw evaluation guidance?There were no indications considered to be flaws found during the RPVH examination.  
      required that plant data be acquired to confirm the head temperature. This data was
11) Did procedures exist to identify potential boric acid leaks from pressure-retainingcomponents above the RPVH?Yes. Procedure 0-PI-DXX-068-100.R, Monitoring of Reactor Head Canopy Seal Weldsfor Leakage, is implemented every outage and meets the requirements of the NRC
      acquired for Unit 1 to satisfy both units because Unit 2 is considered a sister plant. The
Order. However, inspection of conoseals and other bolted connections above the
      inspectors reviewed this data which confirmed that the head operated at approximately
RPVH, such as the RVLIS line, are covered under the Boric Acid Program. The
      cold leg temperature with some minor thermocouple variations. In addition, both units
inspectors determined that the program and procedure implementation met the
      underwent a modification since this testing to increase bypass flow to the head from 4%
requirements of the NRC Order, however, the licensee also initiated actions to enhance
      to about 7%. This gives further assurance that the RPVH operates at cold leg
the method in which compliance with the NRC Order is documented. The inspectors  
      temperature. For these reasons, the inspectors concluded that the licensee had an
reviewed the inspection results for this outage and found that no indications of active or
      adequate basis for their temperature input to the susceptibility ranking calculation, which
recent boric acid leakage from pressure-retaining components above the RPVH were
      results in Unit 2 being placed in the Low category.
identified. 12)Did the licensee perform appropriate follow-on examinations for indications ofboric acid leaks from pressure-retaining components above the RPVH?Yes. The licensee identified some boric acid residue that was later determined bychemical analysis to be older than the recent operating cycle. The residue was
      10)     During non-visual examinations, was the disposition of indications consistent with
attributed to a conoseal leak in 2002. No other indications of boric acid leakage were
              the NRC flaw evaluation guidance?
found during this outage..3(Open) Temporary Instruction (TI) 2515/166, Pressurized Water Reactor ContainmentSump Blockage (NRC Generic Letter 2004-02) - Unit 2    a.Inspection ScopeThe inspectors verified the Unit 2 implementation of the licensee's commitmentsdocumented in their September 1, 2005, response to Generic Letter 2004-02, Potential
      There were no indications considered to be flaws found during the RPVH examination.
Impact of Debris Blockage on Emergency Recirculation During Design Basis Accidents  
      11)     Did procedures exist to identify potential boric acid leaks from pressure-retaining
28Enclosureat Pressurized Water Reactors. The commitments included a permanent screenassembly modification, a license amendment request to change the UFSAR description
              components above the RPVH?
of the sump screen analysis methodology, and submittal of a supplemental response to
      Yes. Procedure 0-PI-DXX-068-100.R, Monitoring of Reactor Head Canopy Seal Welds
GL 2004-02. This review included the sump screen assembly installation procedure,
      for Leakage, is implemented every outage and meets the requirements of the NRC
screen assembly modification 10 CFR 50.59 evaluation, structural (debris) loading
      Order. However, inspection of conoseals and other bolted connections above the
calculation, and validation testing of the modified sump screen design. The inspectors
      RPVH, such as the RVLIS line, are covered under the Boric Acid Program. The
also reviewed the foreign materials exclusion controls and the completed Quality
      inspectors determined that the program and procedure implementation met the
Assurance/Quality Control records for the screen assembly installation. The inspectors
      requirements of the NRC Order, however, the licensee also initiated actions to enhance
conducted a visual walkdown to verify the installed screen assembly configuration was
      the method in which compliance with the NRC Order is documented. The inspectors
consistent with drawings and the tested configuration and verified the design criteria for
      reviewed the inspection results for this outage and found that no indications of active or
screen gap.     b.Findings and ObservationsNo findings of significance were identified.  
      recent boric acid leakage from pressure-retaining components above the RPVH were
Unit 2 permanent modifications completed at the time of this inspection wereimplemented in accordance with Sequoyah Generic Letter 2004-02 response and
      identified.
supporting evaluations. The license amendment request to change the UFSAR screen
      12)     Did the licensee perform appropriate follow-on examinations for indications of
analysis methodology description had been submitted and approved. No modifications
              boric acid leaks from pressure-retaining components above the RPVH?
were required to address downstream effects. TI 2515/166 will remain open pending
      Yes. The licensee identified some boric acid residue that was later determined by
completion and NRC review of the licensee's GL 2004-02 commitments for Unit 1 which
      chemical analysis to be older than the recent operating cycle. The residue was
are scheduled for the fall 2007.  
      attributed to a conoseal leak in 2002. No other indications of boric acid leakage were
 
      found during this outage.
.4(Closed) NRC Temporary Instruction (TI) 2515/169, Mitigating Systems PerformanceIndex (MSPI) Verification     a.Inspection ScopeDuring this inspection period, the inspectors completed a review of the licensee's
.3   (Open) Temporary Instruction (TI) 2515/166, Pressurized Water Reactor Containment
implementation of the Mitigating Systems Performance Index (MSPI) guidance for
      Sump Blockage (NRC Generic Letter 2004-02) - Unit 2
reporting unavailability and unreliability of monitored safety systems in accordance with
   a. Inspection Scope
TI 2515/169. The inspectors examined surveillances that the licensee determined would not renderthe train unavailable for greater than 15 minutes or during which the system could be
      The inspectors verified the Unit 2 implementation of the licensees commitments
promptly restored through operator action and therefore, are not included in
      documented in their September 1, 2005, response to Generic Letter 2004-02, Potential
unavailability calculations. As part of this review, the recovery actions were verified to
      Impact of Debris Blockage on Emergency Recirculation During Design Basis Accidents
be uncomplicated and contained in written procedures.On a sample basis, the inspectors reviewed operating logs, work history information,maintenance rule information, corrective action program documents, and surveillance
                                                                                        Enclosure
procedures to determine the actual time periods the MSPI systems were not available
 
due to planned and unplanned activities. The results were then compared to the
                                                28
baseline planned unavailability and actual planned and unplanned unavailability
      at Pressurized Water Reactors. The commitments included a permanent screen
determined by the licensee to ensure the data's accuracy and completeness. Likewise,
      assembly modification, a license amendment request to change the UFSAR description
these documents were reviewed to ensure MSPI component unreliability data
      of the sump screen analysis methodology, and submittal of a supplemental response to
determined by the licensee identified and properly characterized all failures of monitored
      GL 2004-02. This review included the sump screen assembly installation procedure,
components. The unavailability and unreliability data were then compared with  
      screen assembly modification 10 CFR 50.59 evaluation, structural (debris) loading
29Enclosureperformance indicator data submitted to the NRC to ensure it accurately reflected theperformance history of these systems.    b.Findings and ObservationsNo findings of significance were identified. The licensee accurately documented thebaseline planned unavailability hours, the actual unavailability hours and the actual
      calculation, and validation testing of the modified sump screen design. The inspectors
unreliability information for the MSPI systems. No significant errors in the reported data
      also reviewed the foreign materials exclusion controls and the completed Quality
were identified, which resulted in a change to the indicated index color. No significant
      Assurance/Quality Control records for the screen assembly installation. The inspectors
discrepancies were identified in the MSPI basis document which resulted in: (1) a
      conducted a visual walkdown to verify the installed screen assembly configuration was
change to the system boundary, (2) an addition of a monitored component, or (3) a
      consistent with drawings and the tested configuration and verified the design criteria for
change in the reported index color..5Institute of Nuclear Power Operations (INPO) Plant Assessment Report Review    a.Inspection ScopeThe inspectors reviewed the interim report for the INPO plant assessment report ofSequoyah conducted in July 2006. The inspectors reviewed the report to ensure that
      screen gap.
issues identified were consistent with the NRC perspectives of licensee performance
  b. Findings and Observations
and if any significant safety issues were identified that required further NRC follow-up.    b. FindingsNo findings of significance were identified.
      No findings of significance were identified.
  4OA6Meetings, Including Exit.1Exit Meeting SummaryOn January 3, 2007, the resident inspectors presented the inspection results to
      Unit 2 permanent modifications completed at the time of this inspection were
Mr. R. Douet and other members of his staff, who acknowledged the findings. The
      implemented in accordance with Sequoyah Generic Letter 2004-02 response and
inspectors asked the licensee whether any of the material examined during the
      supporting evaluations. The license amendment request to change the UFSAR screen
inspection should be considered proprietary. No proprietary information was identified.4OA7 Licensee-Identified ViolationsThe following violation of very low safety significance (Green) was identified by thelicensee and is a violation of NRC requirements which meet the criteria of Section VI of
      analysis methodology description had been submitted and approved. No modifications
the NRC Enforcement Policy, NUREG-1600, for being dispositioned as an NCV.*TS 6.8.1 requires that written procedures shall be established, implemented, andmaintained covering the activities recommended in Appendix "A" of Regulatory
      were required to address downstream effects. TI 2515/166 will remain open pending
Guide 1.33, Revision 2, February 1978. Contrary to this, on November 28, 2006,
      completion and NRC review of the licensees GL 2004-02 commitments for Unit 1 which
an AUO improperly implemented 0-GO-13,Reactor Coolant System Drain and
      are scheduled for the fall 2007.
Fill Operations, Revision 54, Appendix AC by mispositioning an RCS loop 4 drainvalve. This revealed itself through the subsequent transfer of RCS inventory to
.4   (Closed) NRC Temporary Instruction (TI) 2515/169, Mitigating Systems Performance
the Reactor Coolant Drain Tank and lowering of RCS pressurizer level. The  
      Index (MSPI) Verification
30Enclosureerror was promptly corrected by operations staff and the event was identified inthe licensee's corrective action program as PER 115534. This finding is of very
  a. Inspection Scope
low safety significance because it did not challenge RCS inventory control by
      During this inspection period, the inspectors completed a review of the licensees
exceeding available makeup capacity.ATTACHMENT: SUPPLEMENTAL INFORMATION  
      implementation of the Mitigating Systems Performance Index (MSPI) guidance for
AttachmentSUPPLEMENTAL INFORMATIONKEY POINTS OF CONTACTLicensee personnel
      reporting unavailability and unreliability of monitored safety systems in accordance with
    J. Adams, Boric AcidD. Bodine, Chemistry/Environmental Manager
      TI 2515/169.
      The inspectors examined surveillances that the licensee determined would not render
      the train unavailable for greater than 15 minutes or during which the system could be
      promptly restored through operator action and therefore, are not included in
      unavailability calculations. As part of this review, the recovery actions were verified to
      be uncomplicated and contained in written procedures.
      On a sample basis, the inspectors reviewed operating logs, work history information,
      maintenance rule information, corrective action program documents, and surveillance
      procedures to determine the actual time periods the MSPI systems were not available
      due to planned and unplanned activities. The results were then compared to the
      baseline planned unavailability and actual planned and unplanned unavailability
      determined by the licensee to ensure the datas accuracy and completeness. Likewise,
      these documents were reviewed to ensure MSPI component unreliability data
      determined by the licensee identified and properly characterized all failures of monitored
      components. The unavailability and unreliability data were then compared with
                                                                                      Enclosure
 
                                                29
      performance indicator data submitted to the NRC to ensure it accurately reflected the
      performance history of these systems.
   b. Findings and Observations
      No findings of significance were identified. The licensee accurately documented the
      baseline planned unavailability hours, the actual unavailability hours and the actual
      unreliability information for the MSPI systems. No significant errors in the reported data
      were identified, which resulted in a change to the indicated index color. No significant
      discrepancies were identified in the MSPI basis document which resulted in: (1) a
      change to the system boundary, (2) an addition of a monitored component, or (3) a
      change in the reported index color.
.5    Institute of Nuclear Power Operations (INPO) Plant Assessment Report Review
   a. Inspection Scope
      The inspectors reviewed the interim report for the INPO plant assessment report of
      Sequoyah conducted in July 2006. The inspectors reviewed the report to ensure that
      issues identified were consistent with the NRC perspectives of licensee performance
      and if any significant safety issues were identified that required further NRC follow-up.
   b. Findings
      No findings of significance were identified.
4OA6 Meetings, Including Exit
.1    Exit Meeting Summary
      On January 3, 2007, the resident inspectors presented the inspection results to
      Mr. R. Douet and other members of his staff, who acknowledged the findings. The
      inspectors asked the licensee whether any of the material examined during the
      inspection should be considered proprietary. No proprietary information was identified.
4OA7 Licensee-Identified Violations
      The following violation of very low safety significance (Green) was identified by the
      licensee and is a violation of NRC requirements which meet the criteria of Section VI of
      the NRC Enforcement Policy, NUREG-1600, for being dispositioned as an NCV.
      *       TS 6.8.1 requires that written procedures shall be established, implemented, and
              maintained covering the activities recommended in Appendix A of Regulatory
              Guide 1.33, Revision 2, February 1978. Contrary to this, on November 28, 2006,
              an AUO improperly implemented 0-GO-13,Reactor Coolant System Drain and
              Fill Operations, Revision 54, Appendix AC by mispositioning an RCS loop 4 drain
              valve. This revealed itself through the subsequent transfer of RCS inventory to
              the Reactor Coolant Drain Tank and lowering of RCS pressurizer level. The
                                                                                        Enclosure
 
                                          30
          error was promptly corrected by operations staff and the event was identified in
          the licensees corrective action program as PER 115534. This finding is of very
          low safety significance because it did not challenge RCS inventory control by
          exceeding available makeup capacity.
ATTACHMENT: SUPPLEMENTAL INFORMATION
                                                                                Enclosure
 
                                  SUPPLEMENTAL INFORMATION
                                    KEY POINTS OF CONTACT
Licensee personnel
J. Adams, Boric Acid
D. Bodine, Chemistry/Environmental Manager
R. Bruno, Training Manager
R. Bruno, Training Manager
R. Douet, Site Vice President
R. Douet, Site Vice President
Line 780: Line 1,379:
S. Tuthill, Chemistry Operations Manager
S. Tuthill, Chemistry Operations Manager
J. Whitaker, ISI
J. Whitaker, ISI
K. Wilkes, Emergency Preparedness ManagerNRC personnel
K. Wilkes, Emergency Preparedness Manager
:R. Bernhard, Region II, Senior Reactor AnalystD. Pickett, Project Manager, Office of Nuclear Reactor RegulationLIST OF ITEMS OPENED, CLOSED, AND DISCUSSEDOpened and Closed05000327,328/2006005-01NCVFailure to Certify Qualifications and Statusof Licensed Operators Were Current and
NRC personnel:
Valid (Section 1R11.3)Opened05000328/2006005-02URIAppendix R Manual Isolation Valve Failureto Close Within the Required Time text
R. Bernhard, Region II, Senior Reactor Analyst
(Section 1R15)
D. Pickett, Project Manager, Office of Nuclear Reactor Regulation
Closed05000327,328/2515/169TIMitigating Systems Performance IndexVerification (Section 4OA5.4)  
                      LIST OF ITEMS OPENED, CLOSED, AND DISCUSSED
A-2Attachment
Opened and Closed
Discussed05000327, 328/2515/150TIReactor Pressure Vessel Head and VesselHead Penetration Nozzles (NRC Order EA-
05000327,328/2006005-01                NCV        Failure to Certify Qualifications and Status
03-009) - Unit 2 (Section 4OA5.2)05000327, 328/2515/166 TIPressurized Water Reactor ContainmentSump Blockage (NRC Generic Letter 2004-
                                                  of Licensed Operators Were Current and
02) - Unit 2 Section 4OA5.3)  
                                                  Valid (Section 1R11.3)
AttachmentLIST OF DOCUMENTS REVIEWEDSection 1R01: Adverse Weather ProtectionSPP-10.14, Freeze Protection, Revision 0M&AI-27, Freeze Protection, Revision 12
Opened
05000328/2006005-02                    URI        Appendix R Manual Isolation Valve Failure
                                                  to Close Within the Required Time text
                                                  (Section 1R15)
Closed
05000327,328/2515/169                  TI        Mitigating Systems Performance Index
                                                  Verification (Section 4OA5.4)
                                                                                      Attachment
 
                          A-2
Discussed
05000327, 328/2515/150 TI    Reactor Pressure Vessel Head and Vessel
                              Head Penetration Nozzles (NRC Order EA-
                              03-009) - Unit 2 (Section 4OA5.2)
05000327, 328/2515/166 TI    Pressurized Water Reactor Containment
                              Sump Blockage (NRC Generic Letter 2004-
                              02) - Unit 2 Section 4OA5.3)
                                                              Attachment
 
                              LIST OF DOCUMENTS REVIEWED
Section 1R01: Adverse Weather Protection
SPP-10.14, Freeze Protection, Revision 0
M&AI-27, Freeze Protection, Revision 12
0-PI-OPS-000-006.0, Freeze Protection, Revision 45
0-PI-OPS-000-006.0, Freeze Protection, Revision 45
1-PI-EFT-234-706.0, Freeze Protection Heat Trace Functional Test, Revision 30 Section 1R02: Evaluation of Changes, Tests, or ExperimentsFull Evaluations:DCN D21640A, Radiation Monitors Are Being Deleted/Abandoned On Unit 1.DCN D21641A, Radiation Monitors Are Being Deleted/Abandoned On Unit 2.
1-PI-EFT-234-706.0, Freeze Protection Heat Trace Functional Test, Revision 30
Section 1R02: Evaluation of Changes, Tests, or Experiments
Full Evaluations:
DCN D21640A, Radiation Monitors Are Being Deleted/Abandoned On Unit 1.
DCN D21641A, Radiation Monitors Are Being Deleted/Abandoned On Unit 2.
DCN D21854A, DG Starting Air PCV Modification.
DCN D21854A, DG Starting Air PCV Modification.
DCN D21247A, Replace The Existing Electrotechnical Controls For The MCR And EBR A/C
DCN D21247A, Replace The Existing Electrotechnical Controls For The MCR And EBR A/C
Condensing Units With Digital Controls.  
Condensing Units With Digital Controls.
DCN D21248A, Replace The Existing Electrotechnical Controls For The MCR And EBR A/C
DCN D21248A, Replace The Existing Electrotechnical Controls For The MCR And EBR A/C
Condensing Units with Digital Controls.
Condensing Units with Digital Controls.
FSAR Section 15.2.10, Revision to Section 15.2.10 of the FSAR containing the transientanalysis for feed water malfunction event.
FSAR Section 15.2.10, Revision to Section 15.2.10 of the FSAR containing the transient
analysis for feed water malfunction event.
TACF 1-05-013-R1, Temporary configuration change involving installation of non-nuclear safety
TACF 1-05-013-R1, Temporary configuration change involving installation of non-nuclear safety
low volume high pressure pump into the SI System.  
low volume high pressure pump into the SI System.
TACF 1-05-002-063, R1, Temporary installation of TVA Class B piping/tubing and check valve
TACF 1-05-002-063, R1, Temporary installation of TVA Class B piping/tubing and check valve
downstream of 1-VLV-63-834 to provide RHRS pressure relief leakage.
downstream of 1-VLV-63-834 to provide RHRS pressure relief leakage.
FSAR Section 10.4.7 and 10.4.8, Proposed FSAR change to allow Steam Generator Blowdown
FSAR Section 10.4.7 and 10.4.8, Proposed FSAR change to allow Steam Generator Blowdown
to remain in service for various reasons.
to remain in service for various reasons.
ES-1.3, R12, Revised ES-1.3 to modify guidance on stopping and restarting SI pump (PER 04-
ES-1.3, R12, Revised ES-1.3 to modify guidance on stopping and restarting SI pump (PER 04-
000344-000). Screened Out Items:1-SI-OPS-000-003.M R32, Add Glycol Valves In Accordance With 06-NSS-061-035.TI-28 REV 198, Procedure Revision On Unit 1 NIS Power Range Calibration Data  
000344-000).
Screened Out Items:
1-SI-OPS-000-003.M R32, Add Glycol Valves In Accordance With 06-NSS-061-035.
TI-28 REV 198, Procedure Revision On Unit 1 NIS Power Range Calibration Data
0-SI-OPS-068-137.0, Added Precaution And Limitation G To Section 3.2.
0-SI-OPS-068-137.0, Added Precaution And Limitation G To Section 3.2.
0-SO-14-4 Rev 10, Added Section 8.5 To Provide Instructions For Manual Operation Of
0-SO-14-4 Rev 10, Added Section 8.5 To Provide Instructions For Manual Operation Of
Line 811: Line 1,440:
0-SO-77-11 R15, Revised To Add A Precaution To Monitor Waste Gas Vent Header
0-SO-77-11 R15, Revised To Add A Precaution To Monitor Waste Gas Vent Header
Frequently.
Frequently.
1-SO-63-1, Rev. 45, Revised section 8.1 step 6 of procedure to make the step conditional.
1-SO-63-1, Rev. 45, Revised section 8.1 step 6 of procedure to make the step conditional.
2-SI-OPS-000-003.M, Rev. 26, Added note 5 to exempt monthly valve stroke of the glycol valve
2-SI-OPS-000-003.M, Rev. 26, Added note 5 to exempt monthly valve stroke of the glycol valve
when the valve was stroked in the previous 7 days.  
when the valve was stroked in the previous 7 days.
0-GO-14-4, R12, Revised to incorporate changes in accordance with NB 060785.
0-GO-14-4, R12, Revised to incorporate changes in accordance with NB 060785.
0-GO-5, Rev. 47, Revised step in section 5.4 concerning control rods, ref. NB 060297; added
0-GO-5, Rev. 47, Revised step in section 5.4 concerning control rods, ref. NB 060297; added
step to section 5.1 concerning MFPT master controller output, ref. PER 100196-03.
step to section 5.1 concerning MFPT master controller output, ref. PER 100196-03.
1-AR-M1-A, Rev. 38, Revised in response to 060738 which provided additional information
1-AR-M1-A, Rev. 38, Revised in response to 060738 which provided additional information
regarding the inputs for Window A-5.
regarding the inputs for Window A-5.
DCN D20960A, Sequoyah Independent Spent Fuel Storage Installation, (ISFSI).
DCN D20960A, Sequoyah Independent Spent Fuel Storage Installation, (ISFSI).
0-SO-30-10, R31, Revised section 8.15 to provide guidance for Auxiliary Building Chill Water
0-SO-30-10, R31, Revised section 8.15 to provide guidance for Auxiliary Building Chill Water
Feed and Bleed when system is set up for winter operation.  
Feed and Bleed when system is set up for winter operation.
A-4Attachment2-SI-TDC-068-254, Rev. 5, Surveillance instruction is being changed from 18 months toconditional.  
                                                                                  Attachment
 
                                                  A-4
2-SI-TDC-068-254, Rev. 5, Surveillance instruction is being changed from 18 months to
conditional.
0-SO-70-1, R34, Added a step and caution to sections 8.5.2 and 8.5.4 to initiate a Work Order
0-SO-70-1, R34, Added a step and caution to sections 8.5.2 and 8.5.4 to initiate a Work Order
to backfill affected flow transmitter following restoration of CCCS HX. 0B1 or 0B2 after
to backfill affected flow transmitter following restoration of CCCS HX. 0B1 or 0B2 after
maintenance.
maintenance.
0-SO-77-1, Rev.40, Revised to provide guidance on the transfer of the Laundry and Hot
0-SO-77-1, Rev.40, Revised to provide guidance on the transfer of the Laundry and Hot
Shower Tank to the CDCT; moved guidance on re-circulation of the CDCT to new appendix E.  
Shower Tank to the CDCT; moved guidance on re-circulation of the CDCT to new appendix E.
1-SI-OPS-000-003.M, R33, Revise note 18 in Appendix A of surveillance instruction to show
1-SI-OPS-000-003.M, R33, Revise note 18 in Appendix A of surveillance instruction to show
allowable channel deviation of less than or equal to 5%. Problem Evaluation Reports (PERs):84897, 0-PI-ECC-313-595.0 Cannot Be Performed As Currently Written31739, Westinghouse Advisory Letter NASL-02-3 Describes A Process Measurement Uncertain
allowable channel deviation of less than or equal to 5%.
Problem Evaluation Reports (PERs):
84897, 0-PI-ECC-313-595.0 Cannot Be Performed As Currently Written
31739, Westinghouse Advisory Letter NASL-02-3 Describes A Process Measurement Uncertain
99597, Water In Waste Gas Vent Header During Resin Transfer
99597, Water In Waste Gas Vent Header During Resin Transfer
64337, DG 2-PCV-082-262 Blow Down
64337, DG 2-PCV-082-262 Blow Down
Line 836: Line 1,472:
76900, S/G Blowdown Isolation of AFWP Start.
76900, S/G Blowdown Isolation of AFWP Start.
20195, ES 1.3, Transfer to RHR Containment Sump requires stopping the SI Pumps if RCS
20195, ES 1.3, Transfer to RHR Containment Sump requires stopping the SI Pumps if RCS
pressure is greater than 1500 psig. Work Orders:6-771849-000, Check TE Accuracy, if unsatisfactory, Then Replace the TE 6-771384-000, Replace the Oil Cooler TCV for the B MCR ChillerProcedures:TI-28, Rev. 198, Curve Book0-SI-OPS-068-137.0, Rev. 19, Reactor Coolant System Water Inventory
pressure is greater than 1500 psig.
Work Orders:
6-771849-000, Check TE Accuracy, if unsatisfactory, Then Replace the TE
6-771384-000, Replace the Oil Cooler TCV for the B MCR Chiller
Procedures:
TI-28, Rev. 198, Curve Book
0-SI-OPS-068-137.0, Rev. 19, Reactor Coolant System Water Inventory
1-SI-OPS-000-003.M, Rev. 32, Monthly Shift Log
1-SI-OPS-000-003.M, Rev. 32, Monthly Shift Log
1-SI-OPS-000-003.W, Rev. 37, Weekly Shift Log
1-SI-OPS-000-003.W, Rev. 37, Weekly Shift Log
Line 843: Line 1,485:
0-PI-ECC-313-595.0, Rev. 4, Periodic Calibration of Auxiliary Building Heating, Ventilating and
0-PI-ECC-313-595.0, Rev. 4, Periodic Calibration of Auxiliary Building Heating, Ventilating and
Air Conditioning
Air Conditioning
SPP - 9.4, 10 CFR 50.59 Evaluations of Changes, Tests and Experiments, Revision 7.  
SPP - 9.4, 10 CFR 50.59 Evaluations of Changes, Tests and Experiments, Revision 7.
EN-1-102, 10 CFR 50.59 / 10 CFR 72.48, Reviews, Revision 7.Miscellaneous Documents:PMTI-SQN-21854, DG 1A-A Starting Air 5 Start Capacity VerificationSSD 1- L - 68-325, Low RCS Pressurizer Level  
EN-1-102, 10 CFR 50.59 / 10 CFR 72.48, Reviews, Revision 7.
SSD 1 L - 68-326, High RCS Pressurizer Level.
Miscellaneous Documents:
SSD 2 -L -68-325, Low RCS Pressurizer Level  
PMTI-SQN-21854, DG 1A-A Starting Air 5 Start Capacity Verification
SSD 1- L - 68-325, Low RCS Pressurizer Level
SSD 1 L - 68-326, High RCS Pressurizer Level.
SSD 2 -L -68-325, Low RCS Pressurizer Level
SSD 2- L - 68-326, High RCS Pressurizer Level.
SSD 2- L - 68-326, High RCS Pressurizer Level.
NEI 96-07, Nuclear Energy Institute, Guidelines for 10 CFR 50.59 Implementation, Revision 1.
NEI 96-07, Nuclear Energy Institute, Guidelines for 10 CFR 50.59 Implementation, Revision 1.
Regulatory Guide 1.187, Guidance for Implementation of 10 CFR 50.59 Changes, Tests and
Regulatory Guide 1.187, Guidance for Implementation of 10 CFR 50.59 Changes, Tests and
Experiments, November 2000.  
Experiments, November 2000.
A-5AttachmentSection 1R04: Equipment Alignment1,2-47W810-1, Flow Diagram - Residual Heat Removal System, Revision 472-47W811-1, Flow Diagram - SI System, Revision 57Section 1R05: Fire ProtectionSQN Drawing 1,2-47W494-6 Fire Protection Compartmentation-Fire Cells Plan El. 669' & 685'SQN Fire Protection Report Part II - Fire Protection Plan, Revision 20  
                                                                                      Attachment
 
                                              A-5
Section 1R04: Equipment Alignment
1,2-47W810-1, Flow Diagram - Residual Heat Removal System, Revision 47
2-47W811-1, Flow Diagram - SI System, Revision 57
Section 1R05: Fire Protection
SQN Drawing 1,2-47W494-6 Fire Protection Compartmentation-Fire Cells Plan El. 669' & 685'
SQN Fire Protection Report Part II - Fire Protection Plan, Revision 20
SQN-26-D054/EPM-ABB-IMPFHA, SQN Fire Hazards Analysis Calculation, Appendix A
SQN-26-D054/EPM-ABB-IMPFHA, SQN Fire Hazards Analysis Calculation, Appendix A
Spp-10.10, Control of Transient Combustibles, Revision 4Section 1R07: Heat Sink PerformancePER 116021, Containment Spray Heat Exchangers Not in Chemical LayupTVA Letter S64 950922 800, Program Update Regarding NRC GL 89-13 dated September 22,
Spp-10.10, Control of Transient Combustibles, Revision 4
1995
Section 1R07: Heat Sink Performance
1,2-47W812-1, Flow Diagram Containment Spray System, Revision 42Section 1R08: Inservice Inspection Activities
PER 116021, Containment Spray Heat Exchangers Not in Chemical Layup
Programs/Procedures/Reports2-SI-SXI-068-114.3, Steam Generator Tubing Inservice Inspection and Augmented Inspections,Revision 2
TVA Letter S64 950922 800, Program Update Regarding NRC GL 89-13 dated September 22,
1995
1,2-47W812-1, Flow Diagram Containment Spray System, Revision 42
Section 1R08: Inservice Inspection Activities
Programs/Procedures/Reports
2-SI-SXI-068-114.3, Steam Generator Tubing Inservice Inspection and Augmented Inspections,
Revision 2
Degradation Assessment for Sequoyah Unit 2 Cycle 14
Degradation Assessment for Sequoyah Unit 2 Cycle 14
Operational Assessment Report for Unit 2 Cycle 13 Refueling Outage
Operational Assessment Report for Unit 2 Cycle 13 Refueling Outage
Line 870: Line 1,529:
Proc. No. N-UT-64, Rev. 9, Generic Procedure For The UT Examination of Austenitic Pipe
Proc. No. N-UT-64, Rev. 9, Generic Procedure For The UT Examination of Austenitic Pipe
Welds
Welds
Proc. No. N-VT-1, Visual Examination Procedure for ASME Section XI Preservice and Inservice  
Proc. No. N-VT-1, Visual Examination Procedure for ASME Section XI Preservice and Inservice
Proc. No. N-VT-15, Rev. 5, Visual Examination of Class MC and Metallic Liners of Class CC
Proc. No. N-VT-15, Rev. 5, Visual Examination of Class MC and Metallic Liners of Class CC
Components of Light-Water Cooled Plants
Components of Light-Water Cooled Plants
SQN Unit 2 Examination Schedule 0-SI-DXI-115.3, Att.5Design Change Package 22061, Pressurizer Safe End Weld Overlays
SQN Unit 2 Examination Schedule 0-SI-DXI-115.3, Att.5
Design Change Package 22061, Pressurizer Safe End Weld Overlays
WO # 06-775288-002, Pressurizer Safe End Weld Overlays
WO # 06-775288-002, Pressurizer Safe End Weld Overlays
Vendor Instruction 0-VI-MOD-068-001
Vendor Instruction 0-VI-MOD-068-001
Welding Services Traveler 103804-001  
Welding Services Traveler 103804-001
A-6AttachmentCorrective Action (PERS)03-017128-000, NRC inspectors concern that a "GAP" between the support steel and the pipeindicated that the dead weight was not being supported.
                                                                                    Attachment
 
                                              A-6
Corrective Action (PERS)
03-017128-000, NRC inspectors concern that a GAP between the support steel and the pipe
indicated that the dead weight was not being supported.
20732, NRC inspector expressed concern that the NDE procedure N-VT-1 does not address
20732, NRC inspector expressed concern that the NDE procedure N-VT-1 does not address
"GAPS" observed during hanger inspections.
GAPS observed during hanger inspections.
107387, Borated Water Leak on lower flange of 20LCV-62-1`8, Boron is dry
107387, Borated Water Leak on lower flange of 20LCV-62-1`8, Boron is dry
100794, 2A Containment Spray Pump outboard Seal leak.
100794, 2A Containment Spray Pump outboard Seal leak.
106740, Boric Acid Corrosion on support for SQN-2-VLV-063-0578
106740, Boric Acid Corrosion on support for SQN-2-VLV-063-0578
90714, 2-FCV-63-156 packing leak
90714, 2-FCV-63-156 packing leak
81632, Leakage observed on pressurizer safe-ends RCW-25-SE and RCW-26-SE.Section 1R11: Licensed Operator RequalificationQuarterly ReviewAOP-I.08, Turbine Impulse Pressure Instrument Malfunction, Revision 8FR-S.1, Function Restoration Procedure - Nuclear power Generation/ATWS, Revision 20
81632, Leakage observed on pressurizer safe-ends RCW-25-SE and RCW-26-SE.
Section 1R11: Licensed Operator Requalification
Quarterly Review
AOP-I.08, Turbine Impulse Pressure Instrument Malfunction, Revision 8
FR-S.1, Function Restoration Procedure - Nuclear power Generation/ATWS, Revision 20
E-0, Reactor Trip or SI, Revision 27
E-0, Reactor Trip or SI, Revision 27
ES-0.1, Reactor Trip Response, Revision 30Biennial ReviewProcedures and RecordsTRN 11.4 "Continuing Training For Licensed Personnel, Rev. 11.TRN 1 Administering Training, Rev 17.
ES-0.1, Reactor Trip Response, Revision 30
Biennial Review
Procedures and Records
TRN 11.4 Continuing Training For Licensed Personnel, Rev. 11.
TRN 1 Administering Training, Rev 17.
OPDP-1 Conduct of Operations, Appendix 0, License Status-Active/Inactive License, Rev. 6.
OPDP-1 Conduct of Operations, Appendix 0, License Status-Active/Inactive License, Rev. 6.
Operations Directive Manual, Appendix B-Qualifications Tracking Requirements, Rev. 2.
Operations Directive Manual, Appendix B-Qualifications Tracking Requirements, Rev. 2.
Line 896: Line 1,569:
LER 2005-001-00 Units 1 and 2
LER 2005-001-00 Units 1 and 2
LER 2005-002-00 Unit 2
LER 2005-002-00 Unit 2
LER 2006-001-00 Units 1and 2Job Performance MeasuresJPM 163 "Steam line Pressure Transmitter fails low".JPM 33AP "Manual Control of AFW Following a Reactor Trip".
LER 2006-001-00 Units 1and 2
JPM 12 "Pressurizer Level Control Malfunction".
Job Performance Measures
JPM 59 "Establish Excess Letdown".
JPM 163 Steam line Pressure Transmitter fails low.
JPM 80" Local Control of Charging Flow".
JPM 33AP Manual Control of AFW Following a Reactor Trip.
JPM 61A2 "Transfer 480V SD Board 2A1-A From Normal to Alternate Supply".
JPM 12 Pressurizer Level Control Malfunction.
JPM 72 "Local Alignment of 1-RM-90-112 to Lower Containment".
JPM 59 Establish Excess Letdown.
JPM 32AP "Local Manual Control of S/G PORV".
JPM 80" Local Control of Charging Flow.
JPM 6 "Perform Boration of the RCS From Outside the Main Control Room".
JPM 61A2 Transfer 480V SD Board 2A1-A From Normal to Alternate Supply.
JPM 78 AP "Respond to an ATWS Trip the Reactor Locally".  
JPM 72 Local Alignment of 1-RM-90-112 to Lower Containment.
A-7AttachmentSimulator Scenarios:S-13 Uncontrolled Depressurization of All Steam Generators. Rev 12.S-7 Pressurizer Vapor Space Accident. Rev 15.
JPM 32AP Local Manual Control of S/G PORV.
S-11 LOCA with Loss of RHR Recirculation. Rev 13.Simulator Malfunction Tests:ED15 Loss of 250VDC Battery Board.IA03
JPM 6 Perform Boration of the RCS From Outside the Main Control Room.
JPM 78 AP Respond to an ATWS Trip the Reactor Locally.
                                                                                Attachment
 
                                              A-7
Simulator Scenarios:
S-13 Uncontrolled Depressurization of All Steam Generators. Rev 12.
S-7 Pressurizer Vapor Space Accident. Rev 15.
S-11 LOCA with Loss of RHR Recirculation. Rev 13.
Simulator Malfunction Tests:
ED15 Loss of 250VDC Battery Board.
IA03
FW23
FW23
FW20
FW20
ED08
ED08
ED10 Transient Tests:#2 Both Main Feedwater Pumps Trip , AFW fails to start.#5 Trip of Any Single Reactor Coolant Pump.
ED10
Transient Tests:
#2 Both Main Feedwater Pumps Trip , AFW fails to start.
#5 Trip of Any Single Reactor Coolant Pump.
#8 Loop 2 Cold-Leg Large Break LOCA with Loss of Offsite Power.
#8 Loop 2 Cold-Leg Large Break LOCA with Loss of Offsite Power.
#9 Main Steam Line Break Inside Containment.
#9 Main Steam Line Break Inside Containment.
#10 Slow RCS Depressurization to Saturation.Normal Tests:2005 Steady State Operation Drift Test2005 Steady State Operation Static Test for 100%, 66%, and 44% power.Section 1R12: Maintenance EffectivenessTI-4, Maintenance Rule Performance Indicator Monitoring, Trending, and Reporting - 10 CFR50.65, Revision 19Section 1R13: Maintenance Risk Assessments and Emergent Work EvaluationSentinel Run, October 23 to November 12, 2006SQN Plan-of-the-Day, October 26, 2006
#10 Slow RCS Depressurization to Saturation.
Normal Tests:
2005 Steady State Operation Drift Test
2005 Steady State Operation Static Test for 100%, 66%, and 44% power.
Section 1R12: Maintenance Effectiveness
TI-4, Maintenance Rule Performance Indicator Monitoring, Trending, and Reporting - 10 CFR
50.65, Revision 19
Section 1R13: Maintenance Risk Assessments and Emergent Work Evaluation
Sentinel Run, October 23 to November 12, 2006
SQN Plan-of-the-Day, October 26, 2006
SQN MSS-OPS Daily Schedule Report 24 Hour Look-Ahead, October 25, 2006
SQN MSS-OPS Daily Schedule Report 24 Hour Look-Ahead, October 25, 2006
Sentinel Risk Assessment for Failed EDG 2B-BSection 1R15: Operability Evaluations0-SI-SFT-311-001.A, Control Room Air-Conditioning System Train A, Revision 1UFSAR Section 6.4, Habitability Systems
Sentinel Risk Assessment for Failed EDG 2B-B
Section 1R15: Operability Evaluations
0-SI-SFT-311-001.A, Control Room Air-Conditioning System Train A, Revision 1
UFSAR Section 6.4, Habitability Systems
UFSAR Section 9.4, Heating, Ventilating, and Air-Conditioning
UFSAR Section 9.4, Heating, Ventilating, and Air-Conditioning
FE 41643, Observed Air Flow Above Design Flow For MCR 'A" Air Handling Unit
FE 41643, Observed Air Flow Above Design Flow For MCR A Air Handling Unit
1,2-47W866-4, Flow Diagram Heating, Ventilation and Air-Conditioning - Control Building,
1,2-47W866-4, Flow Diagram Heating, Ventilation and Air-Conditioning - Control Building,
Revision 3
Revision 3
1,2-47W867-2, Mechanical Air-Conditioning Control Diagram - Control Building, Revision 12
1,2-47W867-2, Mechanical Air-Conditioning Control Diagram - Control Building, Revision 12
B87 951205 003, ERCW Screen Wash System Hydraulic Analysis, Revisions 2 and 3
B87 951205 003, ERCW Screen Wash System Hydraulic Analysis, Revisions 2 and 3
0-SI-SXP-067-202.B, ERCW Traveling Screen Wash Pump B-B Performance Test, Revision 8  
0-SI-SXP-067-202.B, ERCW Traveling Screen Wash Pump B-B Performance Test, Revision 8
A-8Attachment0-SO-67-1, Essential Raw Cooling Water, Revision 631,2-45N765-1, Wiring Diagram 6900V Shutdown Aux Power Schematic Diagram SH-1,
                                                                                  Attachment
 
                                              A-8
0-SO-67-1, Essential Raw Cooling Water, Revision 63
1,2-45N765-1, Wiring Diagram 6900V Shutdown Aux Power Schematic Diagram SH-1,
Revision 14
Revision 14
1,2-45N765-2, Wiring Diagram 6900V Shutdown Aux Power Schematic Diagram SH-2,
1,2-45N765-2, Wiring Diagram 6900V Shutdown Aux Power Schematic Diagram SH-2,
Line 930: Line 1,633:
1,2-47W809-1, Flow Diagram Chemical & Volume Control System
1,2-47W809-1, Flow Diagram Chemical & Volume Control System
1-108D273-18, Process Control Block Diagram Turbine Impulse Pressure Protection Sets I and
1-108D273-18, Process Control Block Diagram Turbine Impulse Pressure Protection Sets I and
II, Revision 0Section 1R17: Permanent Plant ModificationsProblem Evaluation Reports (PERs):31739, Westinghouse Advisory Letter NASL-02-3 Describes A Process Measurement Uncertain65752, Specified Post Maintenance Testing Deficiencies
II, Revision 0
84070, Diesel Generator 1A-A cable testing.
Section 1R17: Permanent Plant Modifications
Problem Evaluation Reports (PERs):
31739, Westinghouse Advisory Letter NASL-02-3 Describes A Process Measurement Uncertain
65752, Specified Post Maintenance Testing Deficiencies
84070, Diesel Generator 1A-A cable testing.
103766, Main Bank Transformer 1B Hot Spots
103766, Main Bank Transformer 1B Hot Spots
104337, Main Bank Transformer 1B Hot SpotCalculations:Calculation No. SQN- APS - 042, 480 V Turbine Building Common Board Load Coordination,Short Circuit, Circuit Protection and Voltage Drop Analysis, Revision 4.
104337, Main Bank Transformer 1B Hot Spot
Calculation No. SQN-APS-041, 480 VAC Unit Board Load Coordination Study, Revision 4.Work Orders:6-771849-000, Check TE Accuracy, if unsatisfactory, Then Replace the TE 2-002298-000, Westinghouse Advisory Letter NSAL-02-3
Calculations:
Calculation No. SQN- APS - 042, 480 V Turbine Building Common Board Load Coordination,
Short Circuit, Circuit Protection and Voltage Drop Analysis, Revision 4.
Calculation No. SQN-APS-041, 480 VAC Unit Board Load Coordination Study, Revision 4.
Work Orders:
6-771849-000, Check TE Accuracy, if unsatisfactory, Then Replace the TE
2-002298-000, Westinghouse Advisory Letter NSAL-02-3
03-012340-001, Replace degraded portion of 6900 V Diesel Generator 1A-A power cable
03-012340-001, Replace degraded portion of 6900 V Diesel Generator 1A-A power cable
PP351A between Unit 1 Additional Equip. Bldg. And D/G exciter cubicle. 03-012340-002, Install section of new replacement cable PP351A from AEB-1 to MH-14 via
PP351A between Unit 1 Additional Equip. Bldg. And D/G exciter cubicle.
existing conduit. Miscellaneous Documents:Westinghouse Advisory Letter NSAL-03-9ABB Power T&D- Sequoyah Nuclear Plant Final Report "Main Generator Transformer Life
03-012340-002, Install section of new replacement cable PP351A from AEB-1 to MH-14 via
 
existing conduit.
Assessment". Drawings:Drawing No. 1, 2-3591A28, Breaker Setting Sheet 480 V Unit Board 1A, Revision 5Drawing No. 1, 2-3591A30, Breaker Setting Sheet 480 V Unit Board 1B, Revision 6.
Miscellaneous Documents:
Westinghouse Advisory Letter NSAL-03-9
ABB Power T&D- Sequoyah Nuclear Plant Final Report Main Generator Transformer Life
Assessment.
Drawings:
Drawing No. 1, 2-3591A28, Breaker Setting Sheet 480 V Unit Board 1A, Revision 5
Drawing No. 1, 2-3591A30, Breaker Setting Sheet 480 V Unit Board 1B, Revision 6.
Drawing No. 1, 2-3591A32, Breaker Setting Sheet 480 V Unit Board 2A, Revision 6.
Drawing No. 1, 2-3591A32, Breaker Setting Sheet 480 V Unit Board 2A, Revision 6.
Drawing No. 1, 2-3591A34, Breaker Setting Sheet 480 V Unit Board 2B, Revision 5
Drawing No. 1, 2-3591A34, Breaker Setting Sheet 480 V Unit Board 2B, Revision 5
Line 946: Line 1,665:
Drawing No. 1, 2-15E500-3, Transformer Taps and Voltage Limits - Auxiliary Power System,
Drawing No. 1, 2-15E500-3, Transformer Taps and Voltage Limits - Auxiliary Power System,
Revision 16.
Revision 16.
Drawing No. 1-45N1504, Wiring Diagrams - Main Single Line 500 KV Switchyard, Revision 29  
Drawing No. 1-45N1504, Wiring Diagrams - Main Single Line 500 KV Switchyard, Revision 29
A-9AttachmentDrawing No. 1-45W1541, Wiring Diagrams AC Schematic Unit 1 Generator & transformerCircuits, Revision 14Procedures:TI-28, Rev. 198, Curve Book
                                                                                Attachment
PER Written Because of Inspection Finding114743, Superseded ARP revision found in ACR Section 1R19: Post Maintenance TestingPER 115780, 2-FCV-74-28 Did Not Appear To Fully Open2-SI-SXP-074-202.A, RHR Pump 2A-A Performance and Discharge Check Valve Test,
 
                                            A-9
Drawing No. 1-45W1541, Wiring Diagrams AC Schematic Unit 1 Generator & transformer
Circuits, Revision 14
Procedures:
TI-28, Rev. 198, Curve Book
PER Written Because of Inspection Finding
114743, Superseded ARP revision found in ACR
Section 1R19: Post Maintenance Testing
PER 115780, 2-FCV-74-28 Did Not Appear To Fully Open
2-SI-SXP-074-202.A, RHR Pump 2A-A Performance and Discharge Check Valve Test,
Revision 0
Revision 0
WO 06-780773-000, Calibrate 2-FCV-74-28 and Limit SwitchesSection 1R20: Refueling and Outage Activities0-GO-6, Power Reduction from 30& Reactor Power to Hot Standby, Revision 320-GO-7, Unit Shutdown From Hot Standby to Cold Shutdown, Revision 47
WO 06-780773-000, Calibrate 2-FCV-74-28 and Limit Switches
Section 1R20: Refueling and Outage Activities
0-GO-6, Power Reduction from 30& Reactor Power to Hot Standby, Revision 32
0-GO-7, Unit Shutdown From Hot Standby to Cold Shutdown, Revision 47
0-GO-15, Containment Closure Control, Revision 21
0-GO-15, Containment Closure Control, Revision 21
DVD Recording of U2C14 Core Load Verification
DVD Recording of U2C14 Core Load Verification
Line 956: Line 1,688:
Tagout Clearance 2-72-2406-RFO, Motor Operated Valve Maintenance on 2-FCV-72-21
Tagout Clearance 2-72-2406-RFO, Motor Operated Valve Maintenance on 2-FCV-72-21
0-GO-13, Reactor Coolant System Drain and Fill Operations, Revision 54
0-GO-13, Reactor Coolant System Drain and Fill Operations, Revision 54
Sequoyah Nuclear Plant Unit 2 Cycle 15 Core Operating Limits ReportSection 1R22: Surveillance TestingSPP-8.1 Conduct of Testing, Rev 4
Sequoyah Nuclear Plant Unit 2 Cycle 15 Core Operating Limits Report
  Section 1EP6: Drill EvaluationNEI 99-02 Rev 0, March 2000Emergency Plan Implementing Procedure (EPIP) - 1, Emergency Plan Classification Matrix,
Section 1R22: Surveillance Testing
SPP-8.1 Conduct of Testing, Rev 4
Section 1EP6: Drill Evaluation
NEI 99-02 Rev 0, March 2000
Emergency Plan Implementing Procedure (EPIP) - 1, Emergency Plan Classification Matrix,
Rev 37
Rev 37
EPIP-3, Alert, Rev 29
EPIP-3, Alert, Rev 29
Line 963: Line 1,699:
EPIP-5, General Emergency, Rev 36
EPIP-5, General Emergency, Rev 36
EPIP-6, Technical Support Center, Rev 41
EPIP-6, Technical Support Center, Rev 41
EPIP-7, Operations Support Center, Rev 25Section 2OS1: Access Control To Radiologically Significant AreasProcedures, Instructions, Guidance Documents, and Operating ManualsANSI/ANS 3.1-1987, Selection, Qualification, and Training of Personnel for Nuclear PowerPlants
EPIP-7, Operations Support Center, Rev 25
Tennessee Valley Authority (TVA), TVA Nuclear (TVAN), Standard Programs and  
Section 2OS1: Access Control To Radiologically Significant Areas
A-10AttachmentProcesses (SPP) - 3.1, Corrective Action Program, Rev. 11Active Radiation Work Permits (RWPs) List, dated 12/11/2006
Procedures, Instructions, Guidance Documents, and Operating Manuals
ANSI/ANS 3.1-1987, Selection, Qualification, and Training of Personnel for Nuclear Power
Plants
Tennessee Valley Authority (TVA), TVA Nuclear (TVAN), Standard Programs and
                                                                                  Attachment
 
                                                A-10
Processes (SPP) - 3.1, Corrective Action Program, Rev. 11
Active Radiation Work Permits (RWPs) List, dated 12/11/2006
RP Personnel Identification by Craft Report, dated 12/14/2006
RP Personnel Identification by Craft Report, dated 12/14/2006
Task Qualification List (selected individuals), dated December 14, 2006
Task Qualification List (selected individuals), dated December 14, 2006
LHRA Key Control Log Sheets (several pages)  
LHRA Key Control Log Sheets (several pages)
TVA, TVAN, TRN-20, Health Physics Technician Training, Rev. 13
TVA, TVAN, TRN-20, Health Physics Technician Training, Rev. 13
High Radiation Areas at Sequoyah List, document not dated
High Radiation Areas at Sequoyah List, document not dated
SNP RP Organizational Chart (current and proposed changes), document not dated.
SNP RP Organizational Chart (current and proposed changes), document not dated.
TVAN Radiation Protection Peer Team Challenge Update (MS
TVAN Radiation Protection Peer Team Challenge Update (MS Power Point presentation),
Power Point presentation),dated 12/13/2006
dated 12/13/2006
TVA, TVAN, SPP-5.2, ALARA Program, Rev. 3
TVA, TVAN, SPP-5.2, ALARA Program, Rev. 3
RWP 06027010, Rev. 0, Routine Plant Maintenance-Lower Containment All Areas
RWP 06027010, Rev. 0, Routine Plant Maintenance-Lower Containment All Areas
Line 980: Line 1,724:
RWP 06037020, Rev. 0, Inservice Inspection-Steam Generator Primary Side 1-4
RWP 06037020, Rev. 0, Inservice Inspection-Steam Generator Primary Side 1-4
RWP 06047141, Rev. 0, Refueling-U-2 Reactor Cavity
RWP 06047141, Rev. 0, Refueling-U-2 Reactor Cavity
TVA, Sequoyah Nuclear Plant (SNP), Radiological Control Instruction (RCI)-01, RadiationProtection Program
TVA, Sequoyah Nuclear Plant (SNP), Radiological Control Instruction (RCI)-01, Radiation
TVA, SNP, RCI-01, Training and Qualification of Health Physics Technicians-RadiationOperations Technicians, effective date 02/24/05
Protection Program
TVA, SNP, RCI-01, Training and Qualification of Health Physics Technicians-Radiation
Operations Technicians, effective date 02/24/05
TVA, SNP, RCI-14, Radiation Work Permit (RWP) Program, Rev. 37
TVA, SNP, RCI-14, Radiation Work Permit (RWP) Program, Rev. 37
TVA, SNP, RCI-15, Radiological Postings, Rev. 15
TVA, SNP, RCI-15, Radiological Postings, Rev. 15
TVA, SNP, RCI-24, Control of Very High Radiation Areas, Rev. 7
TVA, SNP, RCI-24, Control of Very High Radiation Areas, Rev. 7
TVA, SNP, RCI-28, Control of Locked High Radiation Areas, Rev. 5
TVA, SNP, RCI-28, Control of Locked High Radiation Areas, Rev. 5
TVA, SNP, RCI-29, Control of Radiation Protection Keys, Rev. 4Records and Data ReviewedSNS VSDS Survey Nos. 120506-2, 120606-8, 120506-15, 120606-10, 120606-7, 120706-2,120106-10, 120606-6, and 120306-4
TVA, SNP, RCI-29, Control of Radiation Protection Keys, Rev. 4
Records and Data Reviewed
SNS VSDS Survey Nos. 120506-2, 120606-8, 120506-15, 120606-10, 120606-7, 120706-2,
120106-10, 120606-6, and 120306-4
Air Sample Survey Nos. 120406018, 120506021, 120506024, 120506034, 120506037,
Air Sample Survey Nos. 120406018, 120506021, 120506024, 120506034, 120506037,
120506045, 120506048, 120506053, 120606020, 120706010,120406024, 120606028,
120506045, 120506048, 120506053, 120606020, 120706010,120406024, 120606028,
120506012, and 120606043Corrective Action Program DocumentsNuclear Assurance (NA) - TVAN-Wide - Audit Report No. SSA0502 - Radiological Protectionand Control Audit, dated January 19, 2006
120506012, and 120606043
Corrective Action Program Documents
Nuclear Assurance (NA) - TVAN-Wide - Audit Report No. SSA0502 - Radiological Protection
and Control Audit, dated January 19, 2006
SQN-RP-05-001, Self-Assessment Report, dated 12/22/04
SQN-RP-05-001, Self-Assessment Report, dated 12/22/04
SQN-RP-05-003, Self-Assessment Report, dated 7/29/05
SQN-RP-05-003, Self-Assessment Report, dated 7/29/05
Line 1,000: Line 1,752:
PER 87610, Key Taken Home
PER 87610, Key Taken Home
PER 82027, High Radiation Readings on Valve
PER 82027, High Radiation Readings on Valve
PER 82643, Unexpected Radiation Level Change  
PER 82643, Unexpected Radiation Level Change
A-11AttachmentPER 84532, VHRA Key InventoryPER 99226, Locked High Radiation Door Locks StickingSection 4OA5: Other Activities - Operation of ISFSINEI 96-07, Guidelines for 10 CFR 72.48 Implementation, Appendix BSPP-9.9, 10 CFR 72.48 Evaluations of Changes, Tests, and Experiments for Independent
                                                                                  Attachment
 
                                              A-11
PER 84532, VHRA Key Inventory
PER 99226, Locked High Radiation Door Locks Sticking
Section 4OA5: Other Activities - Operation of ISFSI
NEI 96-07, Guidelines for 10 CFR 72.48 Implementation, Appendix B
SPP-9.9, 10 CFR 72.48 Evaluations of Changes, Tests, and Experiments for Independent
Spent Fuel Storage Installation, Revision 1
Spent Fuel Storage Installation, Revision 1
Regulatory Guide 3.72 - Guidance for Implementation of 10 CFR 72.48, Changes, Tests and
Regulatory Guide 3.72 - Guidance for Implementation of 10 CFR 72.48, Changes, Tests and
Line 1,014: Line 1,773:
10 CFR 48 Screening, Revision to Welding Procedures
10 CFR 48 Screening, Revision to Welding Procedures
10 CFR 48 Screening, Procedure Change to Fuel Handling Instruction FHI-14
10 CFR 48 Screening, Procedure Change to Fuel Handling Instruction FHI-14
10 CFR 48 Screening, Procedure Change to Fuel Handling Instruction FHI-3Section 4OA5: Other Activities - TI 2515/150Procedures0-PI-DXX-068-100.R, Monitoring of Reactor Head Canopy Seal Welds For Leakage, Rev. 154-ISI-603-002, Automated Ultrasonic Examination of RPV Closure Head Penetrations
10 CFR 48 Screening, Procedure Change to Fuel Handling Instruction FHI-3
Section 4OA5: Other Activities - TI 2515/150
Procedures
0-PI-DXX-068-100.R, Monitoring of Reactor Head Canopy Seal Welds For Leakage, Rev. 1
54-ISI-603-002, Automated Ultrasonic Examination of RPV Closure Head Penetrations
Containing Thermal Sleeves
Containing Thermal Sleeves
54-ISI-604-001, Automated Ultrasonic Examination of Open Tube RPV Closure Head
54-ISI-604-001, Automated Ultrasonic Examination of Open Tube RPV Closure Head
Line 1,023: Line 1,786:
N-VT-17, Visual Examination for Leakage of PWR Reactor Head Penetrations, Rev. 4
N-VT-17, Visual Examination for Leakage of PWR Reactor Head Penetrations, Rev. 4
SPP-9.7, Corrosion Control Program, Appendix D, Technical Requirements for the Boric Acid
SPP-9.7, Corrosion Control Program, Appendix D, Technical Requirements for the Boric Acid
Corrosion Control Program, Rev. 13Records/Reports/Engineering DocumentsEquipment Certification Records for the following NDE Equipment:Blade Probes: S1035 NL, S5002 NL, and S5001 NL
Corrosion Control Program, Rev. 13
Ultrasonic Transducers: 21GB-06001 and 2078-06001Engineering Information Record 51-9027415-000, RPV Head Penetration Inspection Plan and
Records/Reports/Engineering Documents
Equipment Certification Records for the following NDE Equipment:
        Blade Probes: S1035 NL, S5002 NL, and S5001 NL
        Ultrasonic Transducers: 21GB-06001 and 2078-06001
Engineering Information Record 51-9027415-000, RPV Head Penetration Inspection Plan and
Coverage Assessment for Sequoyah Units 1 and 2
Coverage Assessment for Sequoyah Units 1 and 2
Calculation C-3217-00-02, Sequoyah 1 and 2 CRDM and Instrument Column Nozzle Stress
Calculation C-3217-00-02, Sequoyah 1 and 2 CRDM and Instrument Column Nozzle Stress
Analysis
Analysis
Letter L44 030227 801, Response to issuance of NRC Order  
Letter L44 030227 801, Response to issuance of NRC Order
A-12AttachmentCorrective Action DocumentsPER 115561, Evidence of leakage during canopy seal weld inspectionPER 116540*, EDY calculation not performed every outage
                                                                                Attachment
 
                                            A-12
Corrective Action Documents
PER 115561, Evidence of leakage during canopy seal weld inspection
PER 116540*, EDY calculation not performed every outage
PER 116165*, Transducer frequencies documented incorrectly
PER 116165*, Transducer frequencies documented incorrectly
*Problem Evaluation Reports generated as a result of this inspectionSection 4OA5: Other Activities - TI 2515/166 Surveillance Instruction 2-SI-SIN-063-009-02, Containment Sump Inspection, dated 11/08/06DCN 22023, Modify Containment Sump Screens as required by NEI Methodology, dated
*Problem Evaluation Reports generated as a result of this inspection
Section 4OA5: Other Activities - TI 2515/166
Surveillance Instruction 2-SI-SIN-063-009-02, Containment Sump Inspection, dated 11/08/06
DCN 22023, Modify Containment Sump Screens as required by NEI Methodology, dated
11/22/06
11/22/06
Amendment to Facility Operating License No. 302, DPR-79, Revised Transport Analysis
Amendment to Facility Operating License No. 302, DPR-79, Revised Transport Analysis
Line 1,050: Line 1,825:
DCN # D22023, "Modify Containment Sump Screens as Required by NEI Methodology", Rev A,
DCN # D22023, "Modify Containment Sump Screens as Required by NEI Methodology", Rev A,
11/22/2006
11/22/2006
Calculation TDI-6009-004, "Module Debris Weight - TVA/Sequoyah -  
Calculation TDI-6009-004, "Module Debris Weight - TVA/Sequoyah - 1/2", Rev 2, 10/13/2006
1/2", Rev 2, 10/13/2006Calculation PCI-5465-S01, "Structural Evaluation of Advanced Design Containment Building
Calculation PCI-5465-S01, "Structural Evaluation of Advanced Design Containment Building
Sump Strainers", Rev 0, 10/20/2006
Sump Strainers", Rev 0, 10/20/2006
Routine Work Order 06-774811-000, "Containment RHR Sump 48N919", Rev 5
Routine Work Order 06-774811-000, "Containment RHR Sump 48N919", Rev 5
FME Accountability Log, SPP 6.5.1Section 4OA5: Other Activities - TI 2515/169Procedures, Manuals, and Guidance DocumentsNEI 99-02, Mitigating System Performance Index (MSPI) Basis Document, Revision 1Selected System Status Reports  
FME Accountability Log, SPP 6.5.1
Section 4OA5: Other Activities - TI 2515/169
Procedures, Manuals, and Guidance Documents
NEI 99-02, Mitigating System Performance Index (MSPI) Basis Document, Revision 1
Selected System Status Reports
0-SI-SXV-063-266.0, ASME Section XI Valve Testing
0-SI-SXV-063-266.0, ASME Section XI Valve Testing
1,2-SI-SXV-000-201.0, Full Stroking of Category "A" and "B" Valves During Operation
1,2-SI-SXV-000-201.0, Full Stroking of Category A and B Valves During Operation
0-SI-SXV-074-266.0, ASME Section XI Valve Testing
0-SI-SXV-074-266.0, ASME Section XI Valve Testing
1,2-SI-OPS-074-128.0, RHR Discharge Piping Vent
1,2-SI-OPS-074-128.0, RHR Discharge Piping Vent
1-SI-SXP-074-074-201.B, RHR Pump 1B-B Performance Test
1-SI-SXP-074-074-201.B, RHR Pump 1B-B Performance Test
2-SI-SXP-074-074-201.B, RHR Pump 1B-B Performance Test
2-SI-SXP-074-074-201.B, RHR Pump 1B-B Performance Test
0-SI-SXV-000-221.0, Full Stroking of the Common ERCW and CCS Category "A" and "B"
0-SI-SXV-000-221.0, Full Stroking of the Common ERCW and CCS Category A and B
Valves During Operation  
Valves During Operation
A-13Attachment0-SI-OPS-067-682.Q, ERCW Non-Safety Related Flow Balance Valve Position Verification0-SI-SXP-067-202.B, ERCW Traveling Screen Wash Pump B-B Performance Test
                                                                                  Attachment
2-SI-OPS-070-32.A, Component Cooling Water Valves Position Verification Train "A"Records and DataSelected Control Room Logs, January 2004 through December 2006EDG NRC Performance Indicators, 2002 - 2005  
 
AFW NRC Performance Indicators, 2002 - 2005  
                                            A-13
HPSI NRC Performance Indicators, 2002 - 2005  
0-SI-OPS-067-682.Q, ERCW Non-Safety Related Flow Balance Valve Position Verification
RHR NRC Performance Indicators, 2002 - 2005  
0-SI-SXP-067-202.B, ERCW Traveling Screen Wash Pump B-B Performance Test
2-SI-OPS-070-32.A, Component Cooling Water Valves Position Verification Train A
Records and Data
Selected Control Room Logs, January 2004 through December 2006
EDG NRC Performance Indicators, 2002 - 2005
AFW NRC Performance Indicators, 2002 - 2005
HPSI NRC Performance Indicators, 2002 - 2005
RHR NRC Performance Indicators, 2002 - 2005
Consolidated Data Entry MSPI Derivation Reports Generated November 2006
Consolidated Data Entry MSPI Derivation Reports Generated November 2006
MSPI Equipment Functional Failure Data Sheets
MSPI Equipment Functional Failure Data Sheets
Maintenance Rule Unavailability Data Sheets, 2002-2006
Maintenance Rule Unavailability Data Sheets, 2002-2006
Maintenance Rule Unreliability Data Sheets, 2002-2006Corrective Action Program DocumentsSelected Corrective Action Reports, 2005-2006  
Maintenance Rule Unreliability Data Sheets, 2002-2006
AttachmentLIST OF ACRONYMS AFWauxiliary feedwaterANSIAmerican National Standards Institute
Corrective Action Program Documents
AOPabnormal operating procedures
Selected Corrective Action Reports, 2005-2006
ARCalternate repair criteria
                                                                                Attachment
ASMEAmerican Society of Mechanical Engineers
 
ATWSanticipated transient without scram
                              LIST OF ACRONYMS
AUOauxiliary unit operator
AFW  auxiliary feedwater
BACCboric acid corrosion control
ANSI  American National Standards Institute
BMVbare metal visual
AOP  abnormal operating procedures
CCPcooling charging pump
ARC  alternate repair criteria
CCPITcooling charging pump injection tank
ASME  American Society of Mechanical Engineers
CFRCode of Federal Regulations
ATWS  anticipated transient without scram
CRcondition report
AUO  auxiliary unit operator
CRDMcontrol rod drive mechanism
BACC  boric acid corrosion control
CVCSchemical volume control system
BMV  bare metal visual
DCNdesign change notice
CCP  cooling charging pump
ECCSemergency core cooling system
CCPIT cooling charging pump injection tank
ECTeddy current testing
CFR  Code of Federal Regulations
EDYeffective degradation years
CR    condition report
ERCWessential raw cooling water
CRDM  control rod drive mechanism
ETSSexamination technique specifications sheet
CVCS  chemical volume control system
FCVflow control valve
DCN  design change notice
FEfunctional evaluation
ECCS  emergency core cooling system
FMEforeign material exclusion
ECT  eddy current testing
FOSARforeign object search and recovery
EDY  effective degradation years
HRhigh radiation
ERCW  essential raw cooling water
HUTholdup tank
ETSS  examination technique specifications sheet
INPOInstitute of Nuclear power Operations
FCV  flow control valve
ISFSIindependent spent fuel storage installation
FE    functional evaluation
ISIinservice inspection
FME  foreign material exclusion
LHRAlocked high radiation area
FOSAR foreign object search and recovery
MRPmaterials reliability program
HR    high radiation
MSPImitigating systems performance index
HUT  holdup tank
NCVnon-cited violation
INPO  Institute of Nuclear power Operations
NDEnon-destructive examination
ISFSI independent spent fuel storage installation
NRCU.S. Nuclear Regulatory Commission
ISI  inservice inspection
ODSCCouter diameter stress corrosion cracking
LHRA  locked high radiation area
OPDPoperations department procedure
MRP  materials reliability program
PARpublically available records
MSPI  mitigating systems performance index
PERproblem evaluation report
NCV  non-cited violation
PERprotective action recommendation
NDE  non-destructive examination
PORVpower-operated relief valve
NRC  U.S. Nuclear Regulatory Commission
PWSCCprimary water stress corrosion cracking
ODSCC outer diameter stress corrosion cracking
RCPreactor coolant pump
OPDP  operations department procedure
RCSreactor coolant system
PAR  publically available records
RHRresidual heat removal
PER  problem evaluation report
RPradiation protection  
PER  protective action recommendation
A-15AttachmentRPVHreactor pressure vessel headRTPrated thermal power
PORV  power-operated relief valve
RWPradiation work permit
PWSCC primary water stress corrosion cracking
RWSTrefueling water storage tank
RCP  reactor coolant pump
SDPsignificance determination process
RCS  reactor coolant system
SERsafety evaluation report
RHR  residual heat removal
SGsteam generator
RP    radiation protection
SIsafety injection
                                                  Attachment
SIsurveillance instructions
 
SSCstructure, system, or component
                                      A-15
TDAFPturbine driven auxiliary feedwater pump
RPVH  reactor pressure vessel head
TItemporary instruction
RTP  rated thermal power
TStechnical specification
RWP  radiation work permit
TVATennessee Valley Authority
RWST  refueling water storage tank
UFSARupdated final safety analysis report
SDP  significance determination process
UHIupper head injection
SER  safety evaluation report
URIunresolved item
SG    steam generator
UTultrasonic testing
SI    safety injection
WOswork orders
SI    surveillance instructions
SSC  structure, system, or component
TDAFP turbine driven auxiliary feedwater pump
TI    temporary instruction
TS    technical specification
TVA  Tennessee Valley Authority
UFSAR updated final safety analysis report
UHI  upper head injection
URI  unresolved item
UT    ultrasonic testing
WOs  work orders
                                              Attachment
}}
}}

Revision as of 10:02, 23 November 2019

(Superceded-see ML070720224) IR 05000327-06-005, IR 05000328-06-005; IR 07200034-06-002; 10/01/06 - 12/31/06; Sequoyah Nuclear Plant, Units 1 & 2; Licensed Operator Requalification Program
ML070300881
Person / Time
Site: Sequoyah  Tennessee Valley Authority icon.png
Issue date: 01/30/2007
From: Widmann M
Reactor Projects Region 2 Branch 6
To: Singer K
Tennessee Valley Authority
References
IR-06-002, IR-06-005
Download: ML070300881 (51)


See also: IR 05000327/2006005

Text

January 30, 2007

Tennessee Valley Authority

ATTN: Mr. Karl W. Singer

Chief Nuclear Officer and

Executive Vice President

6A Lookout Place

1101 Market Street

Chattanooga, TN 37402-2801

SUBJECT: SEQUOYAH NUCLEAR PLANT - NRC INTEGRATED INSPECTION REPORT

05000327/2006005, 05000328/2006005 AND 07200034/2006002

Dear Mr. Singer:

On December 31, 2006, the United States Nuclear Regulatory Commission (NRC) completed

an inspection at your Sequoyah Nuclear Plant, Units 1 and 2. The enclosed integrated

inspection report documents the inspection results, which were discussed on January 3, 2007,

with Mr. R. Duet and other members of your staff.

The inspection examined activities conducted under your licenses as they relate to safety and

compliance with the Commissions rules and regulations and with the conditions of your

licenses. The inspectors reviewed selected procedures and records, observed activities, and

interviewed personnel.

The report documents one NRC-identified finding of very low safety significance. This finding

was determined to involve a violation of NRC requirements. Additionally, a licensee-identified

violation which was determined to be of very low safety significance is listed in this report.

However, because of their very low safety significance and because they are entered into your

corrective action program, the NRC is treating these findings as non-cited violations (NCVs)

consistent with Section VI.A.1 of the NRC Enforcement Policy. If you contest any NCV in this

report, you should provide a response within 30 days of the date of this inspection report, with

the basis for your denial, to the United States Nuclear Regulatory Commission, ATTN.:

Document Control Desk, Washington, D.C. 20555-0001; with copies to the Regional

Administrator Region II; the Director, Office of Enforcement, United States Nuclear Regulatory

Commission, Washington, D.C. 20555-0001; and the NRC Resident Inspector at the Sequoyah

Nuclear Plant.

In accordance with 10 CFR 2.390 of the NRC's "Rules of Practice," a copy of this letter, its

enclosure, and your response (if any) will be available electronically for public inspection in the

NRC Public Document Room or from the Publically Available Records (PARS) component of

2

NRCs document system (ADAMS). ADAMS is accessible from the NRC Website at

http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room).

Sincerely,

/RA/

Malcolm T. Widmann, Chief

Reactor Projects Branch 6

Division of Reactor Projects

Docket Nos.: 50-327, 50-328,72-034

License Nos.: DPR-77, DPR-79

Enclosure: Inspection Report 05000327/2006005 and 05000328/2006005 and

07200034/2006002 w/Attachment: Supplemental Information

cc: w/encl: (See page 3)

____ML070300881 __

OFFICE RII:DRP RII:DRP RII:DRP RII:DRP RII:DRS RII:DRS RII:DRS

SIGNATURE LXG /RA/ WTM /RA/ JBB via email MES via email JXD /RA/ FJE /RA/ LFL /RA/

NAME LGarner MWidmann JBaptist MSpeck JDiaz-Velez FEhrhardt LLake

DATE 01/30/2007 01/30/2007 01/30/2007 01/30/2007 01/30/2007 01/30/2007 01/30/2007

E-MAIL COPY? YES NO YES NO YES NO YES NO YES NO YES NO YES NO

OFFICE RII:DRS RII:DRS RII:DRS RII:DRS RII:DRS RII:DRS RII:DRS

SIGNATURE GWL /RA/ DLM /RA/ ECM /RA/ BWM /RA/ CRO for SDR /RA/ CRO for

NAME GLaska DMasPenaranda EMichel BMiller RMoore SRose CSmith

DATE 01/30/2007 01/30/2007 01/30/2007 01/30/2007 01/30/2007 01/30/2007 01/30/2007

E-MAIL COPY? YES NO YES NO YES NO YES NO YES NO YES NO YES NO

OFFICE RII:DRS

SIGNATURE CRS /RA/

NAME CStancil

DATE 01/30/2007

E-MAIL COPY? YES NO YES NO YES NO YES NO YES NO YES NO YES NO

3

cc w/encls:

Ashok S. Bhatnagar Beth A. Wetzel, Manager

Senior Vice President Corporate Nuclear Licensing and

Nuclear Operations Industry Affairs

Tennessee Valley Authority Tennessee Valley Authority

Electronic Mail Distribution 4X Blue Ridge

1101 Market Street

Preston D. Swafford Chattanooga, TN 37402-2801

Senior Vice President

Nuclear Support Robert H. Bryan, Jr., General Manager

Tennessee Valley Authority Licensing and Industry Affairs

Electronic Mail Distribution Sequoyah Nuclear Plant

Tennessee Valley Authority

Larry S. Bryant, Vice President 4X Blue Ridge

Nuclear Engineering & 1101 Market Street

Technical Services Chattanooga, TN 37402-2801

Tennessee Valley Authority

Electronic Mail Distribution David A. Kulisek, Plant Manager

Sequoyah Nuclear Plant

Randy Douet Tennessee Valley Authority

Site Vice President Electronic Mail Distribution

Sequoyah Nuclear Plant

Electronic Mail Distribution Lawrence E. Nanney, Director

TN Dept. of Environment & Conservation

General Counsel Division of Radiological Health

Tennessee Valley Authority Electronic Mail Distribution

Electronic Mail Distribution

County Mayor

John C. Fornicola, General Manager Hamilton County Courthouse

Nuclear Assurance Chattanooga, TN 37402-2801

Tennessee Valley Authority

Electronic Mail Distribution Ann Harris

341 Swing Loop

Glenn W. Morris, Manager Rockwood, TN 37854

Licensing and Industry Affairs

Sequoyah Nuclear Plant James H. Bassham, Director

Tennessee Valley Authority Tennessee Emergency Management

Electronic Mail Distribution Agency

Electronic Mail Distribution

Distribution w/encl: (See page 4)

4

Letter to Karl W. Singer from Malcolm T. Widmann dated January 30, 2007

SUBJECT: SEQUOYAH NUCLEAR PLANT - NRC INTEGRATED INSPECTION REPORT

05000327/2006005, 05000328/2006005 AND 07200034/2006002

Distribution w/encl:

Bob Pascarelli, NRR

D. Pickett, NRR

C. Evans, RII

L. Slack, RII EICS

OE Mail

RIDSNRRDIRS

PUBLIC

TABLE OF CONTENTS

SUMMARY OF FINDINGS . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 2

REPORT DETAILS . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 3

REACTOR SAFETY . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 3

1R01 Adverse Weather Protection . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 4

1R02 Evaluations of Changes, Tests or Experiments . . . . . . . . . . . . . . . . . . . . . . . . . 4

1R04 Equipment Alignment . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 4

1R05 Fire Protection . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 4

1R07 Heat Sink Performance . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 5

1R08 Inservice Inspection (ISI) Activities . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 6

1R11 Licensed Operator Requalification Program . . . . . . . . . . . . . . . . . . . . . . . . . . . . 9

1R12 Maintenance Effectiveness . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 12

1R13 Maintenance Risk Assessments and Emergent Work Control . . . . . . . . . . . . . 12

1R15 Operability Evaluations . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 13

1R17 Permanent Plant Modifications . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 15

1R19 Post-Maintenance Testing . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 16

1R20 Refueling and Other Outage Activities . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 17

1R22 Surveillance Testing . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 19

1EP6 Drill Evaluation . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 19

RADIATION SAFETY . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 20

2OS1 Access Control To Radiologically Significant Areas . . . . . . . . . . . . . . . . . . . . . 20

OTHER ACTIVITIES . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 21

4OA2 Identification & Resolution of Problems . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 21

4OA5 Other Activities . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 23

4OA6 Management Meetings . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 29

4OA7 Licensee Identified Violations . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 29

ATTACHMENT: SUPPLEMENTARY INFORMATION

Key Points of Contact . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . A-1

List of Items Opened, Closed, and Discussed . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . A-1

List of Documents Reviewed . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . A-3

List of Acronyms . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . A-14

U. S. NUCLEAR REGULATORY COMMISSION

REGION II

Docket Nos: 50-327, 50-328,72-034

License Nos: DPR-77, DPR-79

Report No: 05000327/2006005 and 05000328/2006005 and

07200034/2006002

Licensee: Tennessee Valley Authority (TVA)

Facility: Sequoyah Nuclear Plant

Location: Sequoyah Access Road

Soddy-Daisy, TN 37379

Dates: October 1, 2006 - December 31, 2006

Inspectors: J. Baptist, Acting Senior Resident Inspector

J. Diaz-Velez, Health Physicist (Section 2OS1)

F. Ehrhardt, Operations Engineer (Section 1R11.2)

L. Lake, Reactor Inspector (Section 1R08)

G. Laska, Senior Operations Examiner (Section 1R11.3)

D. Mas-Penaranda, Reactor Inspector (Sections 1R02, 1R17)

E. Michel, Reactor Inspector (Section 4OA5.3)

B. Miller, Reactor Inspector (Sections 1R08, 4OA5.2)

R. Moore, Senior Reactor Inspector (Section 4OA5.3)

S. Rose, Senior Operations Engineer (Section 1R11.3)

C. Smith Senior Reactor Inspector (Sections 1R02, 1R17)

M. Speck, Resident Inspector

C. Stancil, Resident Inspector (Section 1EP6)

Approved by: M. Widmann, Chief

Reactor Projects Branch 6

Division of Reactor Projects

Enclosure

SUMMARY OF FINDINGS

IR 05000327/2006005, IR 05000328/2006005; IR 07200034/2006002; 10/01/2006 -

12/31/2006; Sequoyah Nuclear Plant, Units 1 & 2; Licensed Operator Requalification

Program.

The report covered a three-month period of inspection by resident inspectors and

announced inspections by 10 regional inspectors and one resident inspector from

another site. One NRC-identified Green finding, which was also a non-cited violation,

was identified. The significance of most findings is indicated by their color (Green,

White, Yellow, Red) using Inspection Manual Chapter (IMC) 0609, "Significance

Determination Process" (SDP). Findings for which the SDP does not apply may be

Green or be assigned a severity level after NRC management review. The NRC's

program for overseeing the safe operation of commercial nuclear power reactors is

described in NUREG-1649, "Reactor Oversight Process," Revision 3, dated July 2000.

A. NRC-Identified and Self-Revealing Findings

Cornerstone: Mitigating Systems

Green. The inspectors identified a Green, non-cited violation (NCV) of 10 CFR 55.53,

Conditions of Licenses for failure to certify the qualifications and status of licensed

operators were current and valid prior to their resumption of license duties. Specific

aspects of the requalification program that were not valid included plant tours that were

not completed with another licensed operator and not completing all shift functions in

positions to which the individuals will be assigned. The licensee entered the finding into

the corrective action program as PER No.112004.

The finding is greater than minor because it is associated with the human performance

attribute of the Mitigating Systems Cornerstone that affects the cornerstone objective of

ensuring the availability, reliability, and capability of operators to respond to initiating

events to prevent undesirable consequences that could pose a potential risk to

operations. The finding was evaluated using the Operator Requalification Human

Performance Significance Determination Process. Under this SDP, record deficiencies

can be either minor or of very low safety significance (Green). This finding was

determined to be Green because it was related to the program for maintaining active

licenses and more than 20% of the records reviewed had deficiencies. (Section 1R11.3).

B. Licensee-Identified Violations

A violation of very low safety significance, which was identified by the licensee, was

reviewed by the inspectors. Corrective actions taken or planned by the licensee have

been entered into the licensees corrective action program. This violation and corrective

action are listed in Section 4OA7.

Enclosure

REPORT DETAILS

Summary of Plant Status:

Unit 1 operated at or near 100% rated thermal power (RTP) for the duration of the

reporting period.

Unit 2 operated at or near 100% RTP until November 27, 2006 when it shut down for a

refueling outage. Unit 2 achieved criticality on December 24, 2006, and reached 100%

RTP on December 29, 2006, where it remained for the duration of the reporting period.

1. REACTOR SAFETY

Cornerstones: Initiating Events, Mitigating Systems, and Barrier Integrity

1R01 Adverse Weather Protection

a. Inspection Scope

The inspectors reviewed design features and licensee preparations for protecting the

essential raw cooling water (ERCW) intake structure and both Unit 1 and 2 refueling

water storage tanks (RWSTs) from extreme cold and freezing conditions. The

inspectors reviewed the Updated Final Safety Analysis Report (UFSAR), and Technical

Specifications (TS), reviewed and observed implementation of licensee freeze protection

procedures, and walked down portions of the systems to assess the status of system

deficiencies and the system readiness for extreme cold weather. Inspectors performed

corrective action program keyword searches to verify deficiencies were being identified

at an appropriate level and that actions were taken to correct problems. Documents

reviewed are listed in the Attachment to this report.

b. Findings

No findings of significance were identified.

1R02 Evaluations of Changes, Tests or Experiments

a. Inspection Scope

The inspectors reviewed selected samples of 10 CFR 50.59 evaluations to verify that

the licensee had appropriately considered the conditions under which changes to the

facility, Updated Final Safety Analysis Report (UFSAR), or procedures may be made,

and tests conducted, without prior NRC approval. The inspectors reviewed ten

evaluations completed for changes made by the licensee without prior NRC approval.

The inspectors also reviewed documents prepared in connection with the changes.

Documents reviewed included supporting analyses, the UFSAR, and drawings to verify

that the licensee had correctly concluded that the changes could be made without

obtaining a license amendment. The ten evaluations reviewed are listed in the

Attachment to this report.

Enclosure

4

Additionally, the inspectors reviewed samples of changes for which the licensee had

determined that evaluations were not required. The reviews were performed to verify

that the licensees conclusions to screen out these changes were correct, and the

changes were made in compliance with the requirements of 10 CFR 50.59. The sixteen

screened out changes reviewed are listed in the Attachment to this report.

The inspectors also reviewed selected problem evaluation reports (PERs) to verify that

plant problems were evaluated for root/apparent causes; extent of condition; and that

the developed corrective actions were adequate to ensure recurrence control of the

identified plant problem.

b. Findings

No findings of significance were identified.

1R04 Equipment Alignment

a. Inspection Scope

Partial System Walkdowns. The inspectors performed a partial walkdown of the

following three systems to verify the operability of redundant or diverse trains and

components when safety equipment was inoperable. The inspectors attempted to

identify any discrepancies that could impact the function of the system, and, therefore,

potentially increase risk. The inspectors reviewed applicable operating procedures,

walked down control system components and verified that selected breakers, valves,

and support equipment were in the correct position to support system operation. The

inspectors also verified that the licensee had properly identified and resolved equipment

alignment problems that could cause initiating events or impact the capability of

mitigating systems or barriers and entered them into the corrective action program.

Documents reviewed are listed in the Attachment to this report.

  • Emergency Diesels 1A, 1B, and 2A during diesel 2B Outage
  • Unit 2 Spent Fuel Pool Cooling during full core offload

b. Findings

No findings of significance were identified.

1R05 Fire Protection

a. Inspection Scope

The inspectors conducted a tour of the eight areas listed below to assess the material

condition and operational status of fire protection features. The inspectors verified that

combustibles and ignition sources were controlled in accordance with the licensees

administrative procedures, fire detection and suppression equipment was available for

use; that passive fire barriers were maintained in good material condition; and that

compensatory measures for out-of-service, degraded, or inoperable fire protection

Enclosure

5

equipment were implemented in accordance with the licensees fire plan. Documents

reviewed are listed in the Attachment to this report.

  • Control Building Elevation 669 (Mechanical Equipment Room, 250-VDC Battery

and Battery Board Rooms)

  • Control Building Elevation 706 (Cable Spreading Room)
  • Control Building Elevation 685 (Auxiliary Instrument Rooms)
  • Auxiliary Building Elevation 690 (Corridor)
  • Control Building Elevation 732 (Mechanical Equipment Room and Relay Room)
  • Auxiliary Building Elevation 714 (Corridor)
  • Unit 2 Residual Heat Removal/Containment Spray Heat Exchanger Rooms

The inspectors observed the performance of the site fire brigade during unannounced

drills on March 29, 2006, and September 30, 23006, and reviewed the drill critique

report for an unannounced drill on October 3, 2006, to evaluate the readiness of the fire

brigade to fight fires and to assess the drill against the requirements of the Sequoyah

Nuclear Plant Fire Protection Report, Revision 17. The observed drills simulated fires at

the 480-volt Reactor Motor Operated Valve Board 1B1-B and the Motor-driven Auxiliary

Feedwater Pump 2A-A. The reviewed drill critique was for fire brigade response to a fire

alarm report from the Unit 1 RWST. Specifically, the inspectors reviewed the following

aspects of the drills: use of protective clothing, use of breathing apparatus, proper use

of fire hoses, control of the drill scenario, and recurrence of identified deficiencies.

b. Findings

No findings of significance were identified.

1R07 Heat Sink Performance

a. Inspection Scope

The inspectors observed performance and reviewed the results of the following activity

to verify the heat exchangers readiness and availability. Inspectors interviewed

maintenance and testing personnel and the system engineer, reviewed corrective action

program documents, previous heat exchanger flow rate data, and inspected the heat

exchanger internals for cleanliness. Inspectors also walked down the system while in

operation looking for evidence of leaks following system restoration. Documents

reviewed are listed in the Attachment to this report.

Current Inspection

b. Findings

No findings of significance were identified.

Enclosure

6

1R08 Inservice Inspection (ISI) Activities (71111.08)

.1 Piping and Pressure Boundary Systems ISI

a. Inspection Scope

From December 4 - December 8, 2006, the inspectors observed and reviewed the

licensees implementation of their ISI program for monitoring degradation of the reactor

coolant system (RCS) boundary and other risk significant piping system boundaries for

Unit 2. The inspectors observed and reviewed a sample of American Society of

Mechanical Engineers (ASME),Section XI, Section III, and Risk Informed ISI required

examinations, in order of risk priority, as identified in Section 71111.08-03 of inspection

procedure 71111.08, Inservice Inspection Activities based upon the ISI activities

available for review during the onsite inspection period.

The inspectors conducted an on-site review of nondestructive examination (NDE)

activities to evaluate compliance with TSs and the applicable editions of ASME Section

V and Section XI to verify that indications and defects (if present) were appropriately

evaluated and dispositioned in accordance with the requirements of ASME Section XI

acceptance standards.

The inspectors observed the following examinations:

Manual Ultrasonic Examination:

Visual (VT3) examination of the following Hangers:

  • 2-CVCH-004
  • 2-CVCH-007
  • 2-CVCH-010
  • 2-CVCH-037

Qualification and certification records for examiners, inspection equipment, and

consumables along with the applicable NDE procedures for the above ISI examination

activities were reviewed and compared to requirements stated in ASME Section V and

Section XI.

The inspectors observed in-process welding activities for the following ASME pressure

boundary locations. Inspectors reviewed quality records for welding procedures,

procedure qualification, welder qualification, and filler metal certification.

The inspectors observed a sample of in-process weld-overlay activities for the following

Pressurizer nozzles:

  • Pressurizer Spray Nozzle
  • Pressurizer Surge Nozzle

Enclosure

7

b. Findings

No findings of significance were identified.

.2 Reactor Vessel Upper Head Penetrations

The inspectors completed TI2515/150, Reactor Pressure Vessel Head and Head

Penetration Nozzles (NRC Order EA-03009) (Unit2), this outage. See Section 4OA5.2.

.3 Boric Acid Corrosion Control (BACC) ISI

a. Inspection Scope

The inspectors reviewed the licensees BACC activities to ensure implementation with

commitments made in response to NRC Generic Letter 88-05 Boric Acid Corrosion of

Carbon Steel Reactor Pressure Boundary and Bulletin 2002-01 Reactor Pressure

Vessel Head Degradation and Reactor Coolant Pressure Boundary Integrity.

The inspectors conducted an on-site record review as well as an independent walkdown

of parts of the reactor building that are not normally accessible during at-power

operations to evaluate compliance with licensee BACC program requirements. In

particular, the inspectors assessed whether the visual examinations focused on

locations where boric acid leaks can cause degradation of safety significant components

and that degraded or non-conforming conditions were properly identified in the

licensees corrective action program.

The inspectors reviewed a sample of engineering evaluations completed for boric acid

found on reactor coolant system piping and components. The inspectors also reviewed

licensee corrective actions implemented for evidence of boric acid leakage to confirm

that they were consistent with requirements of Section XI of the ASME Code and 10

CFR 50 Appendix B Criterion XVI.

b. Findings

No findings of significance were identified.

.4 Steam Generator ISI

a. Inspection Scope

From December 11-15, 2006, the inspectors reviewed the Unit 2 Steam Generator (SG)

tube eddy current testing (ECT) examination activities to ensure compliance with TSs,

applicable industry operating experience and technical guidance documents, and ASME

Code Section XI requirements.

The inspectors reviewed licensee SG inspection activities to ensure that ECT

inspections were conducted in accordance with the licensees SG Program and

applicable industry standards. The inspectors reviewed the SG examination scope,

Enclosure

8

ECT acquisition procedures, Examination Technique Specification Sheets (ETSS), ECT

analysis guidelines, the most recent SG degradation assessment and operational

assessment, and also the condition monitoring results as they became available. The

inspectors reviewed documentation to ensure that the ECT probes and equipment

configurations used were qualified to detect the expected types of SG tube degradation.

The inspectors ensured that all tubes evaluated in condition monitoring were

appropriately screened for in-situ testing. No tubes met the criteria for in-situ testing. In

addition, the inspectors ensured that the licensee had appropriately implemented the

NRC-approved Alternate Repair Criteria (ARC) applicable to tubes that experienced

outer diameter stress corrosion cracking (ODSCC) at tube support plates.

The inspectors monitored the licensees secondary side activities, which included a

foreign object search and recovery (FOSAR) for loose parts, and sludge lancing. As

part of an industry commitment, the licensee was required to remove a tube from

service for destructive testing. The inspectors monitored this evolution to ensure there

was no damage to other tubes or other parts of the SG.

b. Findings

No findings of significance were identified.

.5 Identification and Resolution of Problems

a. Inspection Scope

The inspectors performed a review of piping system ISI related problems that were

identified by the licensee and entered into the corrective action program. The inspectors

reviewed corrective action documents to confirm that the licensee had appropriately

described the scope of the problems. Additionally, the inspectors review included

confirmation that the licensee had an appropriate threshold for identifying issues and

had implemented effective corrective actions. The inspectors evaluated the threshold

for identifying issues through interviews with licensee staff and review of licensee

actions to incorporate lessons learned from industry issues related to the ISI program.

The inspectors performed these reviews to ensure compliance with 10 CFR Part 50,

Appendix B, Criterion XVI, Corrective Action, requirements. The corrective action

documents reviewed by the inspectors are listed in the Attachment to this report.

b. Findings

No findings of significance were identified.

Enclosure

9

1R11 Licensed Operator Requalification Program

.1 Quarterly Inspection

a. Inspection Scope

The inspectors observed licensed operator requalification simulator testing on October

24, 2006. The testing involved a failed impulse pressure transmitter failure followed by

loss of condenser vacuum and automatic turbine trip. The reactor failed to automatically

trip and resulted in an anticipated transient without scram (ATWS). The ATWS was

compounded by the inability to trip the reactor from the Main Control Room, auxiliary

feedwater control valves failed to operate automatically for Steam Generators Number 1

and 2, and the Turbine Driven Auxiliary Feedwater Pump (TDAFP) was unable to supply

feedwater, all of which required operator action. As plant conditions were being

stabilized, a pressurizer power operated relief valve (PORV) failed open and required

operators to shut its blocking valve.

The inspectors observed crew performance in terms of communications; ability to take

timely and proper actions; prioritizing, interpreting and verifying alarms; correct use and

implementation of procedures, including the alarm response procedures and emergency

plan event classification; timely control board operation and manipulation, including high

risk operator actions; oversight and direction provided by shift manager, including the

ability to identify and implement appropriate TS actions; independent event classification

by the Shift Technical Advisor; and group dynamics involved in crew performance. The

inspectors also observed the examining staffs assessment of the crews performance

and compared them to inspector observations. Documents reviewed are listed in the

Attachment to this report.

b. Findings

No findings of significance were identified.

.2 Annual Review of Licensee Requalification Examination Results

a. Inspection Scope

On November 17, 2006, the licensee completed the comprehensive requalification

biennial written examinations and annual operating tests required to be given to all

licensed operators by 10 CFR 55.59(a)(2). The inspectors performed an in-office review

of the overall pass/fail results of the written examinations, individual operating tests, and

the crew simulator operating tests. These results were compared to the thresholds

established in Manual Chapter 609 Appendix I, Operator Requalification Human

Performance Significance Determination Process.

b. Findings

No findings of significance were identified.

Enclosure

10

.3 Licensed Operator Requalification Program - Biennial Review

a. Inspection Scope

The inspectors reviewed facility operating history and associated documents in

preparation for this inspection. While onsite the inspectors reviewed documentation,

interviewed licensee personnel, and observed the administration of operating tests and

written examinations associated with the licensees operator requalification program.

Each of the activities performed by the inspectors was done to assess the effectiveness

of the licensee in implementing requalification requirements identified in 10 CFR 55,

Operators Licenses. The evaluations were also performed to determine if the licensee

effectively implemented operator requalification guidelines established in NUREG 1021,

Operator Licensing Examination Standards for Power Reactors, and Inspection

Procedure 71111.11, Licensed Operator Requalification Program. The inspectors also

evaluated the licensees simulation facility for adequacy for use in operator licensing

examinations using ANSI/ANS-3.5-1985, American National Standard for Nuclear

Power Plant Simulators for use in Operator Training and Examination. The inspectors

observed two crews during the performance of the operating tests. Documentation

reviewed included written examinations, job performance measures, simulator

scenarios, licensee procedures, on-shift records, licensed operator qualification records,

watchstanding and medical records, simulator modification request records and

performance test records, the feedback process, and remediation plans. Documents

reviewed during the inspection are listed in the Attachment to this report.

b. Findings

Introduction: A Green NCV was identified for failure to certify that the qualifications and

status of licensed operators were current and valid prior to their resumption of license

duties. The applicable requirements of 10 CFR 55.53, Conditions of Licenses for

license reactivation were not met. Specific aspects of the requalification program that

were not valid included plant tours that were not completed with another licensed

operator and not completing all shift functions in the position to which the individual will

be assigned.

Description: The inspectors identified problems with several aspects of the reactivation

process for licensed operators who had been reactivated between October 1, 2004 and

September 30, 2006. The inspectors performed a detailed review for 5 of the 15

individuals who had licenses reactivated during this time period.

The inspectors identified that complete tours of the plant were not being conducted in

accordance with OPDP-1 Operations Department Procedure, Revision 6 and 10 CFR

55.53 requirements. Some individuals reactivating their licenses were performing the

required plant tours without being accompanied by another licensed individual. The

inspectors also identified that some individuals reactivating their licenses had

documented standing watch in non-TS positions, i.e., those positions that TSs do not

require a licensed operator to fill. 10 CFR 55.53, requires that an authorized

representative of the facility certify that individuals reactivating their license must

complete a minimum of 40 hours4.62963e-4 days <br />0.0111 hours <br />6.613757e-5 weeks <br />1.522e-5 months <br /> of shift functions in the position to which the individual

Enclosure

11

will be assigned and under the direction of a reactor operator or senior reactor operator

as appropriate. The 40 hours4.62963e-4 days <br />0.0111 hours <br />6.613757e-5 weeks <br />1.522e-5 months <br /> shall also include a complete tour of the plant.

The inspectors noted that the licensee performed a self assessment of the licensed

operator requalification program on September 11-26, 2006. The assessment identified

problems in several different areas related to operator license reactivation and

maintenance of active license process. Specifically, one licensed operators reactivation

documents could not be located, two licensed operators were returned to active status

without all required training completed, and one inactive licensed operator assumed

licensed duties without being reactivated.

Analysis: The inspectors determined that the licensees failure to properly certify and

maintain the reactivation records of licensed operators and the failure to perform plant

tours with another licensed operator and complete shift functions in the position to which

the individual will be assigned is a performance deficiency because the licensee must

satisfy the requirements of 10 CFR 55.53 for license reactivation.

The finding is more than minor because it is associated with the human performance

attribute of the Mitigating Systems Cornerstone and adversely affects the cornerstone

objective of ensuring the availability, reliability, and capability of operators to response to

initiating events to prevent undesirable consequences. The failure to properly reactivate

the licenses of operators could adversely impact their performance. The finding was

evaluated using the Operator Requalification Human Performance Significance

Determination Process. Under this SDP, record deficiencies can be either minor or of

very low safety significance (Green). This finding was determined to be Green because

it was related to the program for maintaining active licenses and more than 20% of the

records reviewed had deficiencies.

Enforcement: 10 CFR 55.53.(f) Conditions of Licenses requires, in part, that an

authorized representative of the facility licensee shall certify that qualifications and

status of operator licensees are current and valid prior to the resumption of license

duties. Included in the certification required by 10 CRF 55.53 is that the individual

complete a minimum of 40 hours4.62963e-4 days <br />0.0111 hours <br />6.613757e-5 weeks <br />1.522e-5 months <br /> of shift functions in the position to be assigned and

also complete a plant tour while accompanied by a licensed operator. Contrary to the

above, the licensee did not properly certify that qualifications and status were current

and valid prior to allowing operators to perform licensed duties.

The failure to properly reactivate licensed operators was determined to be of very low

safety significance (Green) and has been entered into the licensees corrective action

program as PER No.112004. The finding is being treated as an NCV consistent with

Section VI.A of the NRC Enforcement Policy: NCV 05000327,328/2006005-01, Failure

to certify qualifications and status of licensed operators were current and valid in

accordance with 10CFR 55.53.

Enclosure

12

1R12 Maintenance Effectiveness

a. Inspection Scope

The inspectors reviewed the following three maintenance activities to verify the

effectiveness of the activities in terms of: 1) appropriate work practices; 2) identifying

and addressing common cause failures; 3) scoping in accordance with 10 CFR 50.65

(b); 4) characterizing reliability issues for performance; 5) trending key parameters for

condition monitoring; 6) charging unavailability for performance; 7) classification in

accordance with 10 CFR 50.65(a)(1) or (a)(2); 8) appropriateness of performance

criteria for Systems, Structures, and Components (SSCs) and functions classified as

(a)(2); and 9) appropriateness of goals and corrective actions for SSCs and functions

classified as (a)(1). Documents reviewed are listed in the Attachment to this report.

  • PER 115421, B-B Main Control Room Ventilation
  • PER 85481, Repeated Packing Leaks of Safety Injection (SI) Valve 2-FCV-63-156

b. Findings

No findings of significance were identified.

1R13 Maintenance Risk Assessments and Emergent Work Control

a. Inspection Scope

The inspectors reviewed the following six activities to verify that the appropriate risk

assessments were performed prior to removing equipment from service for

maintenance. The inspectors verified that risk assessments were performed as

required by 10 CFR 50.65 (a)(4), and were accurate and complete. When emergent

work was performed, the inspectors verified that the plant risk was promptly reassessed

and managed. The inspectors verified the appropriate use of the licensees risk

assessment tool and risk categories in accordance with Procedure SPP-7.1, On-Line

Work Management, Revision 8, and Instruction 0-TI-DSM-000-007.1, Risk Assessment

Guidelines, Revision 8. Documents reviewed are listed in the Attachment to this report.

  • Unit 2 ECCS Train A Room Cooler Outage
  • Unplanned EDG 2B Inoperability
  • ORAM Orange risk condition from Unit 2 midloop activities prior to vacuum refill
  • Unit 2 initial RCS level drain to partial draindown condition

b. Findings

No findings of significance were identified.

Enclosure

13

1R15 Operability Evaluations

a. Inspection Scope

For the five operability evaluations described in the PERs listed below, the inspectors

evaluated the technical adequacy of the evaluations to ensure that TS operability was

properly justified and the subject component or system remained available, such that no

unrecognized increase in risk occurred. The inspectors reviewed the UFSAR to verify

that the system or component remained available to perform its intended function. In

addition, the inspectors reviewed compensatory measures implemented to verify that

the compensatory measures worked as stated and the measures were adequately

controlled. The inspectors also reviewed a sampling of PERs to verify that the licensee

was identifying and correcting any deficiencies associated with operability evaluations.

Documents reviewed are listed in the Attachment to this report.

  • PER 111814, Train A MCR Air-Conditioning System Air Flow Greater Than

Acceptance Criteria

to Close When Required

  • PER 109326, ERCW Screen Wash Pump B-B Failed Pump Performance Test
  • PER 115490, Charging Pump Discharge Manual Isolation Valve Appendix R

Operability

b. Findings

No findings of significance were identified. An unresolved item (URI) is discussed

below.

Inability to Perform Actions Required by AOP-N.08, Appendix R Fire Safe Shutdown

Introduction: The inspectors identified an Unresolved Item (URI) for not promptly

identifying and correcting problems associated with manual valve 2-62-527. These

problems resulted in operators not being able to comply with licensee procedure AOP-

N.08, Appendix R Fire Safe Shutdown due to manual valve 2-62-527 not being able to

be closed within the 13 minutes required.

Description: On October 28, 2005, a procedure change to AOP-N.08, Appendix R Fire

Safe Shutdown, was implemented. This change incorporated updated guidance

provided by a Westinghouse technical bulletin (TB -04-022) concerning RCP seal

performance during Appendix R fires and a loss of all pump seal cooling. This change

reduced the time available to perform manual actions and restore RCP seal flow from 24

minutes to 13 minutes. In the event of an Appendix R fire resulting in a spurious safety

injection signal, plant procedures required that all RCS injection sources be stopped to

prevent filling the pressurizer solid. The vendor guidance stated that actions taken to

prevent this condition and restore RCP seal flow should be completed within 13 minutes

to prevent seal damage. The actions outlined by AOP-N.08 required an auxiliary unit

operator (AUO) to manipulate several valves in the appropriate Charging Pump room

Enclosure

14

and then a CCP restarted to restore seal flow. Specifically, the AUO was to open a

dedicated flow path to the RCP seals using manual valve 62-526 (A-train), or 62-534 (B-

train) and close the associated CCP manual discharge valve,62-527 (A-train) or 62-533

(B-train) to the CCP Injection Tank (CCPIT). To support the procedure change, these

manipulations were subjected to a manual action validation that consisted of a table top

review of the necessary steps. The licensee determined that the CCP manual

discharge valves to the CCPIT could be closed by an individual AUO in 5 minutes and

20 seconds.

Prior to the procedure being approved, PER 91383 was written on October 24, 2005.

The PER addressed concerns by at least one plant AUO that the manual actions

required by the change to procedure AOP-N.08 may not be able to be completed within

the time required. PER 91383 requested the need to further evaluate the time

necessary to perform the manual actions by actual valve manipulations, or whether

additional procedure changes were needed to provide more margin to the required time.

The corrective action planned was to perform a timed valve stroke of CCP discharge

valve 2-62-527 to validate procedural change assumptions. Work Order (WO) 06-

771729-000 was written to implement and track this action during an appropriate CCP

maintenance period. PER 91383 was closed as completed on February 24, 2006 based

on the WO being written. On November 9, 2006, during a self-assessment, the licensee

determined that the WO had not been completed and was not scheduled for

performance until January 22, 2007. PER 114455 was written to document the

incomplete corrective action. Upon review of PER 114455, the inspectors questioned

the licensee on the valves history, the status of corrective actions, and whether a valid

safety concern existed if the valve could not be operated within the prescribed time.

Prior to resolution by the licensee, on November 27, 2006, during Unit 2 refueling

outage activities, operators closed valve 2-62-527 to support maintenance. The

operators reported that the valve was very difficult to operate and required

approximately 30 minutes for two AUOs to shut the valve. This observation was

documented in in PER 115490 and supported the initial concern expressed in PER

91383.

This information prompted the license to evaluate the consequences of the additional

time needed to operate valve 2-62-527 with plant Appendix R procedures. Functional

Evaluation (FE) 41722 was drafted and the licensee determined that RCP seal

degradation would not occur if RCP seal flow was restored with a CCP prior to

completing of the Appendix R Fire safe shutdown manual actions The licensee also

evaluated whether the same problems were likely for other Appendix R manual valves. .

The licensee drafted a document to support the determination that other valves in both

units could be operated in adequate time in the event of an Appendix R fire.

Analysis: The inspectors determined that the delay in implementing the WO resulted in

not promptly identifying and correcting problems with manual valve 2-62-527 resulting in

operators not being able to comply with procedure AOP-N.08, Appendix R Fire Safe

Shutdown. The corrective action for PER 91383 was closed to a WO and rescheduled

several times in the work control process with a performance date of January 22, 2007.

The inspectors referenced Inspection Manual Chapter (IMC) 0612 and determined the

finding is more than minor because if left uncorrected, the licensee would not be able to

Enclosure

15

comply with AOP-N.08. The finding is associated with the mitigating system

cornerstone and could be reasonably viewed as affecting the cornerstone objective to

ensure the availability, reliability, and capability of systems that respond to initiating

events to prevent undesirable consequences. This finding is unresolved pending the

review of supporting documentation and completion of the significance determination.

Enforcement: Pending additional information involving the circumstances surrounding

the event, its extent of condition and completion of the significance determination, this

finding is identified as URI 05000328/2006005-02, Inability to Perform Required Actions

of AOP-N.08, Appendix R Fire Safe Shutdown.

1R17 Permanent Plant Modifications

a. Inspection Scope

The inspectors performed independent design reviews of six plant modifications in the

Initiating Events, Mitigating Systems, and Barrier Integrity cornerstone areas, to verify

that the plant modifications did not have any adverse effects on system availability,

reliability, and functional capability. Documents reviewed included procedures,

engineering calculations, modification design and implementation packages, work

orders, Condition Reports (CRs), applicable sections of the UFSAR, TSs, and design

basis information. The plant modifications and the associated attributes reviewed are as

follows:

DCN D22050, Pressurizer Relief Tank Level Transmitter Removed (Barrier Integrity)

  • Control Signal
  • Energy Needs
  • Process Medium
  • Update of Licensee Documents

DCN D21781, Change Steam Generator Narrow Range Level Transmitter Scaling

(Mitigating System)

  • Control Signal
  • Energy Needs
  • Process Medium
  • Update of Licensee Documents
  • Operations

DCN D21911, Replace Containment Isolation Valve 2-FCV-030-0014(Barrier Integrity)

  • Pressure Boundary
  • Structural
  • Process Medium
  • Update of Licensee Documents
  • Materials/Replacement Components

DCN 21900, Replace Unit 1B Main Bank Transformer and Associated Fire Protection

Ring Header, Revision A.(Initiating Event)

  • Energy Needs
  • Control Signals
  • Post-Installation Testing

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16

  • Update of Licensee Documents
  • Functional Testing Adequacy and Results

DCN D21971, Replace Cable PP351A for D/G 1A-A, Revision A. (Mitigating Systems)

  • Materials/ Replacement
  • Failure Modes
  • Post-Installation Testing
  • Update of Licensee Documents
  • Functional Testing Adequacy and Results

DCN D21827, Revise Setting on Raw Cooling Water Pump Breaker, Revision A.

  • Control Signals
  • Response Time
  • Post-Insulation Testing
  • Update of Licensee Documents
  • Functional Testing Adequacy and Results

The inspectors also performed field inspections of selected plant modifications to verify

that the as-built installation complied with design requirements delineated in approved

design documents. Additionally, the inspectors reviewed selected PERs to verify that

plant problems were evaluated for root/apparent causes, extent of condition, and that

the developed corrective actions were adequate to ensure recurrence control of the

identified plant problem.

b. Findings

No findings of significance were identified.

1R19 Post-Maintenance Testing

a. Inspection Scope

The inspectors reviewed the five post-maintenance tests listed below to verify that

procedures and test activities ensured system operability and functional capability. The

inspectors reviewed the licensees test procedure to verify that the procedure

adequately tested the safety function(s) that may have been affected by the

maintenance activity, that the acceptance criteria in the procedure were consistent with

information in the applicable licensing basis and/or design basis documents, and that

the procedure had been properly reviewed and approved. The inspectors also

witnessed the test or reviewed the test data, to verify that test results adequately

demonstrated restoration of the affected safety function(s). Documents reviewed are

listed in the Attachment to this report.

(AFW) Pump 2B

and Boron Injection Flowpath Valves Via SI Signal, Revision 1

  • WO 05-777912-001, Repack SI system Hot Leg Injection Valve, 2-FCV-63-156

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17

  • WO 06-780773-000, Calibrate FCV and Limit Switches on 2-FCV-074-28

b. Findings

No findings of significance were identified.

1R20 Refueling and Other Outage Activities

a. Inspection Scope

For the Unit 2 refueling outage that began on November 27, 2006, the inspectors

evaluated licensee activities to verify that the licensee considered risk in developing

outage schedules, followed risk reduction methods developed to control plant

configuration, developed mitigation strategies for the loss of key safety functions, and

adhered to operating license and TS requirements that ensure defense-in-depth. The

inspectors also walked down portions of Unit 2 not normally accessible during at-power

operations to verify that safety-related and risk-significant SSCs were maintained in an

operable condition. Specifically, between November 27, 2006, and December 26, 2006,

the inspectors performed inspections and reviews of the following outage activities.

Documents reviewed are listed in the Attachment to this report.

  • Outage Plan. The inspectors reviewed the outage safety plan and contingency

plans to confirm that the licensee had appropriately considered risk, industry

experience, and previous site-specific problems in developing and implementing

a plan that assured maintenance of defense-in-depth.

  • Reactor Shutdown. The inspectors observed the shutdown in the control room

from the time the reactor was tripped until operators placed it on the RHR

system for decay heat removal to verify that TS cooldown restrictions were

followed. The inspectors also toured the lower containment as soon as

practicable after reactor shutdown to observe the general condition of the RCS

and emergency core cooling system components and to look for indications of

previously unidentified leakage inside the polar crane wall.

  • Licensee Control of Outage Activities. On a daily basis, the inspectors attended

the licensee outage turnover meeting, reviewed PERs, and reviewed the

defense-in-depth status sheets to verify that status control was commensurate

with the outage safety plan and in compliance with the applicable TS when

taking equipment out-of-service. The inspectors further toured the main control

room and areas of the plant daily to ensure that the following key safety

functions were maintained in accordance with the outage safety plan and TS:

electrical power, decay heat removal, spent fuel cooling, inventory control,

reactivity control, and containment closure. The inspectors also observed a

tagout of the containment spray heat exchanger to verify that the equipment was

appropriately configured to safely support the work or testing. To ensure that

RCS level instrumentation was properly installed and configured to give accurate

information, the inspectors reviewed the installation of the Mansell level

Enclosure

18

monitoring system. Specifically, the inspectors discussed the system with

engineering, walked it down to verify that it was installed in accordance with

procedures and adequately protected from inadvertent damage, verified that

Mansell indication properly overlapped with pressurizer level instruments during

pressurizer draindown, verified that operators properly set level alarms to

procedurally required setpoints, and verified that the system consistently tracked

while lowering RCS level to reduced inventory conditions. The inspectors also

observed operators compare the Mansell indications with locally-installed

ultrasonic level indicators during entry into mid-loop conditions.

  • Refueling Activities. The inspectors observed fuel movement at the spent fuel

pool and at the refueling cavity in order to verify compliance with TS and that

each assembly was properly tracked from core offload to core reload. In order to

verify proper licensee control of foreign material, the inspectors verified that

personnel were properly checked before entering any foreign material exclusion

(FME) areas, reviewed FME procedures, and verified that the licensee followed

the procedures. To ensure that fuel assemblies were loaded in the core

locations specified by the design, the inspectors independently reviewed the

recording of the licensees final core verification.

  • Reduced Inventory and Mid-Loop Conditions. Prior to the outage, the inspectors

reviewed the licensees commitments to Generic 88-17, Loss of Decay Heat

Removal. Before entering reduced inventory conditions the inspectors verified

that these commitments were in place, that plant configuration was in

accordance with those commitments, and that distractions from unexpected

conditions or emergent work did not affect operator ability to maintain the

required reactor vessel level. While in mid-loop conditions, the inspectors

verified that licensee procedures for closing the containment upon a loss of

decay heat removal were in effect, that operators were aware of how to

implement the procedures, and that other personnel were available to close

containment penetrations if needed.

  • Heatup and Startup Activities. The inspectors toured the containment prior to

reactor startup to verify that debris that could affect the performance of the

containment sump had not been left in the containment. The inspectors

reviewed the licensees mode change checklists to verify that appropriate

prerequisites were met prior to changing TS modes. To verify RCS integrity and

containment integrity, the inspectors further reviewed the licensees RCS

leakage calculations and containment isolation valve lineups. In order to verify

that core operating limit parameters were consistent with core design, the

inspectors also reviewed low power physics testing results and the Core

Operating Limits Report.

b. Findings

No findings of significance were identified.

Enclosure

19

1R22 Surveillance Testing

a. Inspection Scope

For the seven surveillance tests identified below, by witnessing testing and/or reviewing

the test data, the inspectors verified that the SSCs involved in these tests satisfied the

requirements described in the TS surveillance requirements, the UFSAR, applicable

licensee procedures, and that the tests demonstrated that the SSCs were capable of

performing their intended safety functions. Documents reviewed are listed in the

Attachment to this report. Those tests included the following:

  • 1-SI-MIN-061-108.0, Ice Condenser Intermediate Deck Door Weekly Inspection,

Revision 2

  • 2-SI-ICC-090-106.0, Channel Calibration of Containment Building Lower

Compartment Air Monitor 2-R-90-106, Revision 9***

  • 0-SI-MIN-061-109.0, Ice Condenser Intermediate and Lower Inlet Doors and

Vent Curtains, Revision 4*

  • 2-SI-OPS-003-118.0 AFW pump and Valve Auto Actuation, Revision 18

Comprehensive Performance Test, Revision 4**

  • This procedure included an outage ice condenser system surveillance
    • This procedure included inservice testing requirements
      • This procedure included a RCS leakage detection surveillance

b. Findings

No findings of significance were identified.

Cornerstone: Emergency Preparedness

1EP6 Drill Evaluation

a. Inspection Scope

Resident inspectors evaluated the conduct of a routine licensee emergency drill on

October 3, 2006, to identify any weaknesses and deficiencies in classification,

notification, and protective action recommendation (PARs) development activities. The

inspectors observed emergency response operations in the simulated control room to

verify that event classification and notifications were done in accordance with EPIP-1,

Emergency Plan Classification Matrix, Revision 38. The inspectors also attended the

licensee critique of the drill to compare any inspector-observed weakness with those

identified by the licensee in order to verify whether the licensee was properly identifying

failures. Documents reviewed are listed in the Attachment to this report.

Enclosure

20

b. Findings

No findings of significance were identified.

2. RADIATION SAFETY

Cornerstone: Occupational Radiation Safety (OS)

2OS1 Access Control To Radiologically Significant Areas

a. Inspection Scope

Access Control Licensee program activities for monitoring workers and controlling

access to radiologically significant areas and tasks were inspected. The inspector

evaluated procedural guidance; directly observed implementation of administrative and

established physical controls; assessed worker exposures to radiation and radioactive

material; and appraised radiation worker and technician knowledge of, and proficiency

in, the implementation of Radiation Protection (RP) program activities.

During the inspection, radiological controls for ongoing refueling activities for Unit 2 were

observed and discussed. Reviewed tasks included steam generator non-destructive

testing, containment sump modifications, and refueling activities. In addition, licensee

controls for selected tasks scheduled and on-going during the current refueling outage

were assessed. The evaluations included, as applicable, Radiation Work Permit (RWP)

details; use and placement of dosimetry and air sampling equipment; electronic

dosimeter set-points, and monitoring and assessment of worker dose from direct

radiation and airborne radioactivity source terms. Effectiveness of established controls

was assessed against area radiation and contamination survey results, and

occupational doses received. Physical and administrative controls and their

implementation for locked high radiation areas (LHRAs) and very high radiation areas

were evaluated through discussions with cognizant licensee representatives, direct field

observations, and record reviews.

Occupational workers adherence to selected radiation work permits (RWPs) and Health

Physics Technician proficiency in providing job coverage were evaluated through direct

observations of staff performance during job coverage and routine surveillance

activities, review of selected exposure records, and interviews with cognizant licensee

staff. Radiological postings and physical controls for access to designated high

radiation (HRA) and LHRA locations within the Unit 2 Containment, Auxiliary Building,

and Refuel Floor areas were evaluated during facility tours. In addition, the inspectors

independently measured radiation dose rates and evaluated established posting and

access controls for selected Auxiliary Building locations. Occupational exposures

associated with direct radiation and potential radioactive material intakes for were

reviewed and discussed with cognizant licensee representatives.

RP program activities were evaluated against 10 CFR 19.12; 10 CFR 20, Subparts B, C,

F, G, H, and J; UFSAR details in Section 12, RP; TSs Section 6.11, High Radiation

Area; and approved licensee procedures. Licensee procedures, guidance documents,

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21

records, and data reviewed within this inspection area are listed in Section 2OS1 of the

Attachment to this report.

Problem Identification and Resolution Licensee Corrective Action Program documents

associated with access control to radiologically significant areas were reviewed and

assessed. The inspectors evaluated the licensees ability to identify, characterize,

prioritize, and resolve the identified issues in accordance with Standard Programs and

Processes procedure SPP-3.1, Corrective Action Program. Licensee self-assessments

and PER documents related to access control that were reviewed and evaluated in

detail during inspection of this program area are identified in Section 2OS1 of the

Attachment to this report.

The inspector completed 21 of the required 21 samples for Inspection Procedure (IP)

71121.01. All samples have now been completed for this IP.

b. Findings

No findings of significance were identified.

4. OTHER ACTIVITIES

4OA2 Identification and Resolution of Problems

.1 Daily Review

As required by Inspection Procedure 71152, Identification and Resolution of Problems,

and in order to help identify repetitive equipment failures or specific human performance

issues for follow-up, the inspectors performed a daily screening of items entered into the

licensees corrective action program. This was accomplished by reviewing the

description of each new PER and attending daily management review committee

meetings.

.2 Semi-Annual Trend Review

a. Inspection Scope

As required by Inspection Procedure 71152, the inspectors performed a review of the

licensees corrective action program and associated documents to identify trends that

could indicate the existence of a more significant safety issue. The inspectors review

was focused on procedure quality and compliance issues, but also included licensee

trending efforts and licensee human performance results. The inspectors review

nominally considered the six-month period of July 2006 through December 2006,

although some examples expanded beyond those dates when the scope of the trend

warranted.

Specifically, the inspectors consolidated the results of daily inspector screening

discussed in Section 4OA2.1 into a log, reviewed the log, and compared it to licensee

integrated quarterly trend reports for the period from July 2006 through September 2006

Enclosure

22

in order to determine the existence of any adverse trends that the licensee may not

have previously identified.

b. Assessment and Observations

The inspectors identified issues with procedure quality and compliance over the period

of assessment. Noteworthy examples of deficient procedure quality or compliance

were:

  • PER 114003, Incorrect Procedure Revision used on 6.9kV Shutdown Board relay

testing

  • PER 115490, Inability to manually operate Appendix R valves within the required

time.

failure of Unit 2 Phase A testing requirements.

  • PER 115534, Loss of RCS inventory during Unit 2 refueling outage Mansell

alignment.

  • PER 117008, Missed firewatch through plant areas with disabled fire detection.

No findings of significance were identified. In general, the licensee had identified trends

and appropriately communicated them to plant senior management. The inspectors

evaluated the licensee trending methodology and observed that the licensee had

performed a summary review of issues which were inputs to the plant Human

Performance Index. The licensee reviewed cause codes, involved organizations, key

words, and system links to identify potential trends in the data. The inspectors

compared the licensee process results with the results of the inspectors daily

screenings and did not identify any significant discrepancies or potential trends that the

licensee had failed to identify. The specifics surrounding PER 115490, regarding the

inability to manually operate Appendix R valves within the required time, are further

addressed in Section 1R15, Operability Evaluations.

.3 Annual Sample Review of Problems with Plant Venting Operations

a. Inspection Scope

The inspectors reviewed licensee actions to resolve issues surrounding plant venting

operations. This review began as a look at how the licensee addressed problems

associated with two potentially significant events that had occurred during the venting of

plant systems. These events are common to nuclear plant operations and often are

required in restoration of a system after it has been removed from service or opened for

maintenance. PER 92485 was written on November 21, 2005, and identified that

operators had discovered the collapse of the A Chemical Volume Control System

(CVCS) Holdup Tank (HUT) due to the lack of an adequate vent path during drain down.

The licensee subsequently suspended use of the A CVCS HUT, performed a root

cause analysis, and implemented corrective actions to prevent a recurrence of this

activity. The inspectors reviewed the completion of required actions items spawned

from this event for timeliness, accuracy and adequacy. PER 102591 was written on

May 7, 2006, to address an event during drain down of the RCS to midloop conditions.

While making preparations for vacuum refill of the RCS, the evolution had to be

Enclosure

23

suspended when it was identified that a required reactor vessel head vent path was not

properly aligned. The licensee immediately vented the RCS and verified that the RCS

was not under vacuum conditions based on no observed change in RCS level indication

when the head vent was opened. The licensee declared that the apparent cause of the

event was due to failure to follow procedure, inadequate procedural guidance, and

inadequate scheduling. The event associated with PER 102591 was dispositioned as a

licensee-identified violation in Inspection Report 05000327, 328/2006003. The

inspectors reviewed the PER action items for adequacy and the associated procedures

to ensure changes were implemented to preclude repetition of this event. The

inspectors utilized these examples during the inspection period to observe similar

activities that had the potential to degrade in risk significant systems. The inspectors

were able to observe RCS drain down and refill activities during the Unit 2 Cycle 14

refueling outage, as well as, the venting operations of support systems during

restoration to their normal mode of operation.

b. Findings and Observations

No findings of significance were identified. The inspectors noted that the licensee

appeared to have an adequate sensitivity to operational experience, procedural

guidance, scheduling conflicts, and foreign material exclusion. The licensee was

successful in properly performing the necessary venting activities associated with the

multiple system drain and refill operations accompanying Unit 2 refueling outage

maintenance.

4OA5 Other Activities

.1 Review of the Operation of an Independent Spent Fuel Storage Installation (ISFSI)

(60855.1)

a. Inspection Scope

The inspectors reviewed ISFSI document control practices to verify that changes to the

required ISFSI procedures and equipment were performed in accordance with

guidelines established in licensee procedures and 10 CFR 72.48. Documents reviewed

are listed in the Attachment to this report.

b. Findings

No findings of significance were identified.

.2 (Open) NRC Temporary Instruction 2515/150, Rev. 2, Reactor Pressure Vessel Head

and Vessel Head Penetration Nozzles (NRC Order EA-03-009) - Unit 2

a. Inspection Scope

From December 4 - 8, 2006, the inspectors reviewed the licensees activities associated

with the NDE of the reactor pressure vessel head (RPVH) penetration nozzles, the bare

metal visual examination of the top surface of the RPVH, and the visual examination to

identify potential boric acid leaks from pressure-retaining components above the RPVH.

Enclosure

24

These activities were performed in response to NRC Bulletins 2001-01, 2002-01, 2002-

02, and the first revision of NRC Order EA-03-009 Modifying Licenses dated February

20, 2004 (hereafter referred to as the NRC Order).

The inspectors review of the NDE of RPVH penetration nozzles included independent

observation and evaluation of ultrasonic testing (UT) examinations (for both data

acquisition and analysis), review of NDE procedures, personnel qualifications and

training, and NDE equipment certifications. The inspectors also held interviews with

contractor representatives (Areva) and other licensee personnel involved with the RPVH

examination. The activities were reviewed to verify licensee compliance with the NRC

Order and to gather information to help the NRC staff identify possible further regulatory

positions and generic communications.

The inspectors reviewed a sample of the results from the volumetric UT examinations of

RPVH penetration nozzles. Specifically, the inspectors reviewed or observed the

following:

  • Observed in-process UT data acquisition scanning of RPVH penetration nozzles

57 and 52 (both with thermal sleeves)

  • Reviewed the UT electronic data with the Level III analyst for RPVH nozzles 4,

36, 43, 50, 56, 61, 69, 77, 126 and the calibration block (this included nozzles

both with and without thermal sleeves)

  • Reviewed the results of the UT examination performed to assess for leakage into

the annulus (interference fit zone) between the RPVH penetration nozzle and the

RPVH low-alloy steel for all penetration numbers listed in the previous bullet

  • Reviewed the procedures and results for the visual exam performed to identify

potential boric acid leaks from pressure-retaining components above the RPVH

  • Reviewed the RPVH susceptibility ranking and calculation of effective

degradation years (EDY), including the basis for the RPVH temperature used in

the calculation

b. Observations and Findings

In accordance with the requirements of TI 2515/150, the inspectors evaluated and

answered the following questions:

1) Were the examinations performed by qualified and knowledgeable personnel?

Yes. All personnel involved with the RPVH inspections were appropriately qualified in

accordance with the ASME Code, and most far exceeded the minimum requirements for

experience and training hours. The contractor (Areva) personnel responsible for

equipment manipulation, data acquisition, and data analysis frequently perform these

types of inspections nationwide.

Enclosure

25

2) Were the examinations performed in accordance with demonstrated

procedures?

Yes. The Sequoyah Unit 2 RPVH has 57 control rod drive mechanism (CRDM) nozzles

with thermal sleeves, 13 with open housings (including 5 instrument column nozzles), 8

with part lengths, 4 upper head injection (UHI) nozzles, and 1 vent line nozzle, for a total

of 83 nozzles. All nozzles were subject to remote automated UT examination using one

of two types of probes. The blade probe was used for sleeved penetrations and the

open housing CRDMs using a dummy sleeve. The rotating probe was used for the

other open housing penetrations (UHI and instrument columns). A liquid penetrant

exam on the surface of the J-groove weld of the vent line was also performed to satisfy

the NRC Order.

Procedures 54-ISI-603-002 (UT with thermal sleeves), 54-ISI-604-001 (UT of open

housings), 54-ISI-605-02 (UT of vent line), and 54-ISI-240-44 (liquid penetrant) were

implemented to complete the exams described above. Further, the inspectors verified

that the 54-ISI-603-002 and 54-ISI-604-001 procedures were used during the Areva

demonstration to EPRIs Materials Reliability Program (MRP) to show flaw detection

capability in RPVH penetrations. By letter dated October 3, 2006, from Jack Spanner of

EPRI to Joel Whitaker of TVA (the licensee), EPRI stated that Arevas demonstration of

flaw detection techniques could reliably detect flaws in CRDM penetrations.

3) Was the examination able to identify, disposition, and resolve deficiencies?

Yes. All indications of cracks or interference fit zone leakage are required to be

reported for further examination and disposition. Based on observation of the

examination process, the inspectors considered deficiencies would be appropriately

identified, dispositioned, and resolved. UT indications associated with the geometry of

the examined volume were identified in several penetration tubes. None of the

indications exhibited crack-like characteristics and were appropriately dispositioned in

accordance with procedures.

4) Was the examination capable of identifying the primary water stress corrosion

cracking (PWSCC) and/or RPVH corrosion phenomena described in the NRC

Order?

Yes. The NDE techniques employed for the examination of RPVH nozzles had been

previously demonstrated under the EPRI MRP/Inspection Demonstration Program as

capable of detecting PWSCC-type manufactured cracks as well as cracks from actual

samples from another site. Based on the demonstration, observation of in-process

examinations, and review of NDE data, the inspectors determined that the licensee was

capable of identifying PWSCC and/or corrosion as required by the NRC Order.

5) What was the physical condition of the RPVH (e.g. debris, insulation, dirt, boron

from other sources, physical layout, viewing obstructions)?

The licensee performed a 100% bare metal visual (BMV) inspection of the top of the

RPVH, including 360E around each penetration using a remote visual robotic crawler for

areas inside the lead shielding and underneath the raised insulation package. The

Enclosure

26

surface sloping down from the shielding to the flange was visually inspected directly by a

Level III VT-2 examiner. The inspectors independently reviewed portions of the remote

inspection video which revealed no insulation, dirt, or other general debris that caused

viewing obstructions in the areas of interest. Some small, loose particles of debris were

easily cleared from the surface with a low-pressure air stream mounted on the remote

crawler. The inspectors determined that the physical condition of the head was

adequate to meet the inspection requirements mandated by the NRC Order.

6) Could small boron deposits, as described in NRC Bulletin 2001-01, be identified

and characterized?

Yes. The BMV examination was determined by the inspectors to be capable of

identifying and characterizing small boron deposits as described in NRC Bulletin 2001-

01. The remote exam was VT-2 qualified and able to resolve, at a minimum, the 0.105-

inch characters on an ASME IWA-2210-1 Visual Illumination Card.

7) What material deficiencies (i.e., cracks, corrosion, etc.) were identified that

required repair?

There were no identified examples of RPVH penetration cracks, leakage, material

deficiencies, head corrosion, or other flaws that required repair. As discussed

previously, there were some UT indications at J-groove welds that were dispositioned as

metallurgical/geometric indications (not service related). One metallurgical indication on

tube 56 actually extended below the J-groove weld, and the inspector verified that

adequate coverage below this metallurgical indication was obtained. These indications

were likely due to weld repairs performed during initial RPVH fabrication.

8) What, if any, impediments to effective examinations, for each of the applied

methods, were identified (e.g., centering rings, insulation, thermal sleeves,

instrumentation, nozzle distortion)?

The penetration nozzles with thermal sleeves and centering pads did not impede

effective examination. Concerning examination coverage, the NRC Order requires that

each tubes volume is inspected from a minimum of 2 inches above the highest point of

the J-groove weld to 2 inches below the lowest point of the J-groove weld, or 1 inch with

a stress analysis. The licensee had performed a stress analysis and the inspectors

verified that the minimum examination coverages required by the NRC Order were met.

9) What was the basis for the temperature used in the susceptibility ranking

calculation?

NRC Order EA-03-009 requires that licensees calculate the EDY of the RPVH to

determine its susceptibility category, which subsequently determines the scope and

frequency of required RPVH examinations. The operating temperature of the RPVH is

an input to this calculation. Therefore, an incorrect temperature input could result in

placing the RPVH in an incorrect susceptibility category. The licensee uses the cold leg

temperature in this calculation.

Enclosure

27

In Supplement No. 1 to the NRCs Safety Evaluation Report (SER) dated February

1980, the NRC concluded that scale model tests provided reasonable assurance that

the upper head would operate at the cold leg temperature. However, the NRC staff also

required that plant data be acquired to confirm the head temperature. This data was

acquired for Unit 1 to satisfy both units because Unit 2 is considered a sister plant. The

inspectors reviewed this data which confirmed that the head operated at approximately

cold leg temperature with some minor thermocouple variations. In addition, both units

underwent a modification since this testing to increase bypass flow to the head from 4%

to about 7%. This gives further assurance that the RPVH operates at cold leg

temperature. For these reasons, the inspectors concluded that the licensee had an

adequate basis for their temperature input to the susceptibility ranking calculation, which

results in Unit 2 being placed in the Low category.

10) During non-visual examinations, was the disposition of indications consistent with

the NRC flaw evaluation guidance?

There were no indications considered to be flaws found during the RPVH examination.

11) Did procedures exist to identify potential boric acid leaks from pressure-retaining

components above the RPVH?

Yes. Procedure 0-PI-DXX-068-100.R, Monitoring of Reactor Head Canopy Seal Welds

for Leakage, is implemented every outage and meets the requirements of the NRC

Order. However, inspection of conoseals and other bolted connections above the

RPVH, such as the RVLIS line, are covered under the Boric Acid Program. The

inspectors determined that the program and procedure implementation met the

requirements of the NRC Order, however, the licensee also initiated actions to enhance

the method in which compliance with the NRC Order is documented. The inspectors

reviewed the inspection results for this outage and found that no indications of active or

recent boric acid leakage from pressure-retaining components above the RPVH were

identified.

12) Did the licensee perform appropriate follow-on examinations for indications of

boric acid leaks from pressure-retaining components above the RPVH?

Yes. The licensee identified some boric acid residue that was later determined by

chemical analysis to be older than the recent operating cycle. The residue was

attributed to a conoseal leak in 2002. No other indications of boric acid leakage were

found during this outage.

.3 (Open) Temporary Instruction (TI) 2515/166, Pressurized Water Reactor Containment

Sump Blockage (NRC Generic Letter 2004-02) - Unit 2

a. Inspection Scope

The inspectors verified the Unit 2 implementation of the licensees commitments

documented in their September 1, 2005, response to Generic Letter 2004-02, Potential

Impact of Debris Blockage on Emergency Recirculation During Design Basis Accidents

Enclosure

28

at Pressurized Water Reactors. The commitments included a permanent screen

assembly modification, a license amendment request to change the UFSAR description

of the sump screen analysis methodology, and submittal of a supplemental response to

GL 2004-02. This review included the sump screen assembly installation procedure,

screen assembly modification 10 CFR 50.59 evaluation, structural (debris) loading

calculation, and validation testing of the modified sump screen design. The inspectors

also reviewed the foreign materials exclusion controls and the completed Quality

Assurance/Quality Control records for the screen assembly installation. The inspectors

conducted a visual walkdown to verify the installed screen assembly configuration was

consistent with drawings and the tested configuration and verified the design criteria for

screen gap.

b. Findings and Observations

No findings of significance were identified.

Unit 2 permanent modifications completed at the time of this inspection were

implemented in accordance with Sequoyah Generic Letter 2004-02 response and

supporting evaluations. The license amendment request to change the UFSAR screen

analysis methodology description had been submitted and approved. No modifications

were required to address downstream effects. TI 2515/166 will remain open pending

completion and NRC review of the licensees GL 2004-02 commitments for Unit 1 which

are scheduled for the fall 2007.

.4 (Closed) NRC Temporary Instruction (TI) 2515/169, Mitigating Systems Performance

Index (MSPI) Verification

a. Inspection Scope

During this inspection period, the inspectors completed a review of the licensees

implementation of the Mitigating Systems Performance Index (MSPI) guidance for

reporting unavailability and unreliability of monitored safety systems in accordance with

TI 2515/169.

The inspectors examined surveillances that the licensee determined would not render

the train unavailable for greater than 15 minutes or during which the system could be

promptly restored through operator action and therefore, are not included in

unavailability calculations. As part of this review, the recovery actions were verified to

be uncomplicated and contained in written procedures.

On a sample basis, the inspectors reviewed operating logs, work history information,

maintenance rule information, corrective action program documents, and surveillance

procedures to determine the actual time periods the MSPI systems were not available

due to planned and unplanned activities. The results were then compared to the

baseline planned unavailability and actual planned and unplanned unavailability

determined by the licensee to ensure the datas accuracy and completeness. Likewise,

these documents were reviewed to ensure MSPI component unreliability data

determined by the licensee identified and properly characterized all failures of monitored

components. The unavailability and unreliability data were then compared with

Enclosure

29

performance indicator data submitted to the NRC to ensure it accurately reflected the

performance history of these systems.

b. Findings and Observations

No findings of significance were identified. The licensee accurately documented the

baseline planned unavailability hours, the actual unavailability hours and the actual

unreliability information for the MSPI systems. No significant errors in the reported data

were identified, which resulted in a change to the indicated index color. No significant

discrepancies were identified in the MSPI basis document which resulted in: (1) a

change to the system boundary, (2) an addition of a monitored component, or (3) a

change in the reported index color.

.5 Institute of Nuclear Power Operations (INPO) Plant Assessment Report Review

a. Inspection Scope

The inspectors reviewed the interim report for the INPO plant assessment report of

Sequoyah conducted in July 2006. The inspectors reviewed the report to ensure that

issues identified were consistent with the NRC perspectives of licensee performance

and if any significant safety issues were identified that required further NRC follow-up.

b. Findings

No findings of significance were identified.

4OA6 Meetings, Including Exit

.1 Exit Meeting Summary

On January 3, 2007, the resident inspectors presented the inspection results to

Mr. R. Douet and other members of his staff, who acknowledged the findings. The

inspectors asked the licensee whether any of the material examined during the

inspection should be considered proprietary. No proprietary information was identified.

4OA7 Licensee-Identified Violations

The following violation of very low safety significance (Green) was identified by the

licensee and is a violation of NRC requirements which meet the criteria of Section VI of

the NRC Enforcement Policy, NUREG-1600, for being dispositioned as an NCV.

  • TS 6.8.1 requires that written procedures shall be established, implemented, and

maintained covering the activities recommended in Appendix A of Regulatory

Guide 1.33, Revision 2, February 1978. Contrary to this, on November 28, 2006,

an AUO improperly implemented 0-GO-13,Reactor Coolant System Drain and

Fill Operations, Revision 54, Appendix AC by mispositioning an RCS loop 4 drain

valve. This revealed itself through the subsequent transfer of RCS inventory to

the Reactor Coolant Drain Tank and lowering of RCS pressurizer level. The

Enclosure

30

error was promptly corrected by operations staff and the event was identified in

the licensees corrective action program as PER 115534. This finding is of very

low safety significance because it did not challenge RCS inventory control by

exceeding available makeup capacity.

ATTACHMENT: SUPPLEMENTAL INFORMATION

Enclosure

SUPPLEMENTAL INFORMATION

KEY POINTS OF CONTACT

Licensee personnel

J. Adams, Boric Acid

D. Bodine, Chemistry/Environmental Manager

R. Bruno, Training Manager

R. Douet, Site Vice President

B. Dungan, Outage and Site Scheduling Manager

J. Epperson, Licensed Operator Requal Lead

J. Goulart, ISI

K. Jones, Site Engineering Manager

Z. Kitts, Licensing Engineer

D. Kulisek, Plant Manager

G. Morris, Licensing and Industry Affairs Manager

T. Niessen, Site Quality Manager

M. A. Palmer, Radiation Protection Manager

M. H. Palmer, Operations Manager

K. Parker, Maintenance and Modifications Manager

J. Proffitt, (Acting) Site Licensing Supervisor

J. Reisenbuechler, Operations Training Manager

R. Reynolds, Site Security Manager

N. Thomas, Licensing Engineer

S. Tuthill, Chemistry Operations Manager

J. Whitaker, ISI

K. Wilkes, Emergency Preparedness Manager

NRC personnel:

R. Bernhard, Region II, Senior Reactor Analyst

D. Pickett, Project Manager, Office of Nuclear Reactor Regulation

LIST OF ITEMS OPENED, CLOSED, AND DISCUSSED

Opened and Closed

05000327,328/2006005-01 NCV Failure to Certify Qualifications and Status

of Licensed Operators Were Current and

Valid (Section 1R11.3)

Opened

05000328/2006005-02 URI Appendix R Manual Isolation Valve Failure

to Close Within the Required Time text

(Section 1R15)

Closed

05000327,328/2515/169 TI Mitigating Systems Performance Index

Verification (Section 4OA5.4)

Attachment

A-2

Discussed

05000327, 328/2515/150 TI Reactor Pressure Vessel Head and Vessel

Head Penetration Nozzles (NRC Order EA-

03-009) - Unit 2 (Section 4OA5.2)

05000327, 328/2515/166 TI Pressurized Water Reactor Containment

Sump Blockage (NRC Generic Letter 2004-

02) - Unit 2 Section 4OA5.3)

Attachment

LIST OF DOCUMENTS REVIEWED

Section 1R01: Adverse Weather Protection

SPP-10.14, Freeze Protection, Revision 0

M&AI-27, Freeze Protection, Revision 12

0-PI-OPS-000-006.0, Freeze Protection, Revision 45

1-PI-EFT-234-706.0, Freeze Protection Heat Trace Functional Test, Revision 30

Section 1R02: Evaluation of Changes, Tests, or Experiments

Full Evaluations:

DCN D21640A, Radiation Monitors Are Being Deleted/Abandoned On Unit 1.

DCN D21641A, Radiation Monitors Are Being Deleted/Abandoned On Unit 2.

DCN D21854A, DG Starting Air PCV Modification.

DCN D21247A, Replace The Existing Electrotechnical Controls For The MCR And EBR A/C

Condensing Units With Digital Controls.

DCN D21248A, Replace The Existing Electrotechnical Controls For The MCR And EBR A/C

Condensing Units with Digital Controls.

FSAR Section 15.2.10, Revision to Section 15.2.10 of the FSAR containing the transient

analysis for feed water malfunction event.

TACF 1-05-013-R1, Temporary configuration change involving installation of non-nuclear safety

low volume high pressure pump into the SI System.

TACF 1-05-002-063, R1, Temporary installation of TVA Class B piping/tubing and check valve

downstream of 1-VLV-63-834 to provide RHRS pressure relief leakage.

FSAR Section 10.4.7 and 10.4.8, Proposed FSAR change to allow Steam Generator Blowdown

to remain in service for various reasons.

ES-1.3, R12, Revised ES-1.3 to modify guidance on stopping and restarting SI pump (PER 04-

000344-000).

Screened Out Items:

1-SI-OPS-000-003.M R32, Add Glycol Valves In Accordance With 06-NSS-061-035.

TI-28 REV 198, Procedure Revision On Unit 1 NIS Power Range Calibration Data

0-SI-OPS-068-137.0, Added Precaution And Limitation G To Section 3.2.

0-SO-14-4 Rev 10, Added Section 8.5 To Provide Instructions For Manual Operation Of

Temporary Sump Pump.

0-SO-77-11 R15, Revised To Add A Precaution To Monitor Waste Gas Vent Header

Frequently.

1-SO-63-1, Rev. 45, Revised section 8.1 step 6 of procedure to make the step conditional.

2-SI-OPS-000-003.M, Rev. 26, Added note 5 to exempt monthly valve stroke of the glycol valve

when the valve was stroked in the previous 7 days.

0-GO-14-4, R12, Revised to incorporate changes in accordance with NB 060785.

0-GO-5, Rev. 47, Revised step in section 5.4 concerning control rods, ref. NB 060297; added

step to section 5.1 concerning MFPT master controller output, ref. PER 100196-03.

1-AR-M1-A, Rev. 38, Revised in response to 060738 which provided additional information

regarding the inputs for Window A-5.

DCN D20960A, Sequoyah Independent Spent Fuel Storage Installation, (ISFSI).

0-SO-30-10, R31, Revised section 8.15 to provide guidance for Auxiliary Building Chill Water

Feed and Bleed when system is set up for winter operation.

Attachment

A-4

2-SI-TDC-068-254, Rev. 5, Surveillance instruction is being changed from 18 months to

conditional.

0-SO-70-1, R34, Added a step and caution to sections 8.5.2 and 8.5.4 to initiate a Work Order

to backfill affected flow transmitter following restoration of CCCS HX. 0B1 or 0B2 after

maintenance.

0-SO-77-1, Rev.40, Revised to provide guidance on the transfer of the Laundry and Hot

Shower Tank to the CDCT; moved guidance on re-circulation of the CDCT to new appendix E.

1-SI-OPS-000-003.M, R33, Revise note 18 in Appendix A of surveillance instruction to show

allowable channel deviation of less than or equal to 5%.

Problem Evaluation Reports (PERs):

84897, 0-PI-ECC-313-595.0 Cannot Be Performed As Currently Written

31739, Westinghouse Advisory Letter NASL-02-3 Describes A Process Measurement Uncertain

99597, Water In Waste Gas Vent Header During Resin Transfer

64337, DG 2-PCV-082-262 Blow Down

98255, MCR B Chiller Oil Temperature Swinging

65752, Specified Post Maintenance Testing Deficiencies

76900, S/G Blowdown Isolation of AFWP Start.

20195, ES 1.3, Transfer to RHR Containment Sump requires stopping the SI Pumps if RCS

pressure is greater than 1500 psig.

Work Orders:

6-771849-000, Check TE Accuracy, if unsatisfactory, Then Replace the TE

6-771384-000, Replace the Oil Cooler TCV for the B MCR Chiller

Procedures:

TI-28, Rev. 198, Curve Book

0-SI-OPS-068-137.0, Rev. 19, Reactor Coolant System Water Inventory

1-SI-OPS-000-003.M, Rev. 32, Monthly Shift Log

1-SI-OPS-000-003.W, Rev. 37, Weekly Shift Log

0-SO-14-4, Rev. 10, Condensate Demineralizer waste Disposal

0-SO-77-11, Rev. 15, Waste Gas Compressor Operation

0-PI-ECC-313-595.0, Rev. 4, Periodic Calibration of Auxiliary Building Heating, Ventilating and

Air Conditioning

SPP - 9.4, 10 CFR 50.59 Evaluations of Changes, Tests and Experiments, Revision 7.

EN-1-102, 10 CFR 50.59 / 10 CFR 72.48, Reviews, Revision 7.

Miscellaneous Documents:

PMTI-SQN-21854, DG 1A-A Starting Air 5 Start Capacity Verification

SSD 1- L - 68-325, Low RCS Pressurizer Level

SSD 1 L - 68-326, High RCS Pressurizer Level.

SSD 2 -L -68-325, Low RCS Pressurizer Level

SSD 2- L - 68-326, High RCS Pressurizer Level.

NEI 96-07, Nuclear Energy Institute, Guidelines for 10 CFR 50.59 Implementation, Revision 1.

Regulatory Guide 1.187, Guidance for Implementation of 10 CFR 50.59 Changes, Tests and

Experiments, November 2000.

Attachment

A-5

Section 1R04: Equipment Alignment

1,2-47W810-1, Flow Diagram - Residual Heat Removal System, Revision 47

2-47W811-1, Flow Diagram - SI System, Revision 57

Section 1R05: Fire Protection

SQN Drawing 1,2-47W494-6 Fire Protection Compartmentation-Fire Cells Plan El. 669' & 685'

SQN Fire Protection Report Part II - Fire Protection Plan, Revision 20

SQN-26-D054/EPM-ABB-IMPFHA, SQN Fire Hazards Analysis Calculation, Appendix A

Spp-10.10, Control of Transient Combustibles, Revision 4

Section 1R07: Heat Sink Performance

PER 116021, Containment Spray Heat Exchangers Not in Chemical Layup

TVA Letter S64 950922 800, Program Update Regarding NRC GL 89-13 dated September 22,

1995

1,2-47W812-1, Flow Diagram Containment Spray System, Revision 42

Section 1R08: Inservice Inspection Activities

Programs/Procedures/Reports

2-SI-SXI-068-114.3, Steam Generator Tubing Inservice Inspection and Augmented Inspections,

Revision 2

Degradation Assessment for Sequoyah Unit 2 Cycle 14

Operational Assessment Report for Unit 2 Cycle 13 Refueling Outage

Self Assessment CRP-ENG-009 SQN ASME Section XI Program

Self Assessment 06SQN-12-ENG-XI ASME Section XI Inservice Inspection (ISI) Program

SQN-ENG-03-007 Boric Acid Program Effectiveness Assessment

SPP-9.7, Corrosion Control Program, Rev. 13

Technical Instruction 0-TI-DXX-000-097.1, Rev. 01, Boric Acid Corrosion Control Program

BP-257, Rev. 5, TVA Business Practice, Integrated Material Issues Management Plan,

Appendix A

Proc. No. N-UT-76, Rev. 6, Generic Procedure for Ultrasonic Examination of Ferritic Pipe

Welds.

Proc. No. N-UT-64, Rev. 9, Generic Procedure For The UT Examination of Austenitic Pipe

Welds

Proc. No. N-VT-1, Visual Examination Procedure for ASME Section XI Preservice and Inservice

Proc. No. N-VT-15, Rev. 5, Visual Examination of Class MC and Metallic Liners of Class CC

Components of Light-Water Cooled Plants

SQN Unit 2 Examination Schedule 0-SI-DXI-115.3, Att.5

Design Change Package 22061, Pressurizer Safe End Weld Overlays

WO # 06-775288-002, Pressurizer Safe End Weld Overlays

Vendor Instruction 0-VI-MOD-068-001

Welding Services Traveler 103804-001

Attachment

A-6

Corrective Action (PERS)

03-017128-000, NRC inspectors concern that a GAP between the support steel and the pipe

indicated that the dead weight was not being supported.

20732, NRC inspector expressed concern that the NDE procedure N-VT-1 does not address

GAPS observed during hanger inspections.

107387, Borated Water Leak on lower flange of 20LCV-62-1`8, Boron is dry

100794, 2A Containment Spray Pump outboard Seal leak.

106740, Boric Acid Corrosion on support for SQN-2-VLV-063-0578

90714, 2-FCV-63-156 packing leak

81632, Leakage observed on pressurizer safe-ends RCW-25-SE and RCW-26-SE.

Section 1R11: Licensed Operator Requalification

Quarterly Review

AOP-I.08, Turbine Impulse Pressure Instrument Malfunction, Revision 8

FR-S.1, Function Restoration Procedure - Nuclear power Generation/ATWS, Revision 20

E-0, Reactor Trip or SI, Revision 27

ES-0.1, Reactor Trip Response, Revision 30

Biennial Review

Procedures and Records

TRN 11.4 Continuing Training For Licensed Personnel, Rev. 11.

TRN 1 Administering Training, Rev 17.

OPDP-1 Conduct of Operations, Appendix 0, License Status-Active/Inactive License, Rev. 6.

Operations Directive Manual, Appendix B-Qualifications Tracking Requirements, Rev. 2.

Badge Access Transaction Reports

Licensed Operator Medical Records

Remedial Training Records

Written Exams: A3 RO Exam and A3 SRO Exam.

Simulator Work Request - PR4542

LER 2005-001-00 Units 1 and 2

LER 2005-002-00 Unit 2

LER 2006-001-00 Units 1and 2

Job Performance Measures

JPM 163 Steam line Pressure Transmitter fails low.

JPM 33AP Manual Control of AFW Following a Reactor Trip.

JPM 12 Pressurizer Level Control Malfunction.

JPM 59 Establish Excess Letdown.

JPM 80" Local Control of Charging Flow.

JPM 61A2 Transfer 480V SD Board 2A1-A From Normal to Alternate Supply.

JPM 72 Local Alignment of 1-RM-90-112 to Lower Containment.

JPM 32AP Local Manual Control of S/G PORV.

JPM 6 Perform Boration of the RCS From Outside the Main Control Room.

JPM 78 AP Respond to an ATWS Trip the Reactor Locally.

Attachment

A-7

Simulator Scenarios:

S-13 Uncontrolled Depressurization of All Steam Generators. Rev 12.

S-7 Pressurizer Vapor Space Accident. Rev 15.

S-11 LOCA with Loss of RHR Recirculation. Rev 13.

Simulator Malfunction Tests:

ED15 Loss of 250VDC Battery Board.

IA03

FW23

FW20

ED08

ED10

Transient Tests:

  1. 2 Both Main Feedwater Pumps Trip , AFW fails to start.
  1. 5 Trip of Any Single Reactor Coolant Pump.
  1. 8 Loop 2 Cold-Leg Large Break LOCA with Loss of Offsite Power.
  1. 9 Main Steam Line Break Inside Containment.
  1. 10 Slow RCS Depressurization to Saturation.

Normal Tests:

2005 Steady State Operation Drift Test

2005 Steady State Operation Static Test for 100%, 66%, and 44% power.

Section 1R12: Maintenance Effectiveness

TI-4, Maintenance Rule Performance Indicator Monitoring, Trending, and Reporting - 10 CFR 50.65, Revision 19

Section 1R13: Maintenance Risk Assessments and Emergent Work Evaluation

Sentinel Run, October 23 to November 12, 2006

SQN Plan-of-the-Day, October 26, 2006

SQN MSS-OPS Daily Schedule Report 24 Hour Look-Ahead, October 25, 2006

Sentinel Risk Assessment for Failed EDG 2B-B

Section 1R15: Operability Evaluations

0-SI-SFT-311-001.A, Control Room Air-Conditioning System Train A, Revision 1

UFSAR Section 6.4, Habitability Systems

UFSAR Section 9.4, Heating, Ventilating, and Air-Conditioning

FE 41643, Observed Air Flow Above Design Flow For MCR A Air Handling Unit

1,2-47W866-4, Flow Diagram Heating, Ventilation and Air-Conditioning - Control Building,

Revision 3

1,2-47W867-2, Mechanical Air-Conditioning Control Diagram - Control Building, Revision 12

B87 951205 003, ERCW Screen Wash System Hydraulic Analysis, Revisions 2 and 3

0-SI-SXP-067-202.B, ERCW Traveling Screen Wash Pump B-B Performance Test, Revision 8

Attachment

A-8

0-SO-67-1, Essential Raw Cooling Water, Revision 63

1,2-45N765-1, Wiring Diagram 6900V Shutdown Aux Power Schematic Diagram SH-1,

Revision 14

1,2-45N765-2, Wiring Diagram 6900V Shutdown Aux Power Schematic Diagram SH-2,

Revision 20

WO 04-774974-000, Replace Emergency Diesel Generator 2B-B Breaker

1,2-47W809-1, Flow Diagram Chemical & Volume Control System

1-108D273-18, Process Control Block Diagram Turbine Impulse Pressure Protection Sets I and

II, Revision 0

Section 1R17: Permanent Plant Modifications

Problem Evaluation Reports (PERs):

31739, Westinghouse Advisory Letter NASL-02-3 Describes A Process Measurement Uncertain

65752, Specified Post Maintenance Testing Deficiencies

84070, Diesel Generator 1A-A cable testing.

103766, Main Bank Transformer 1B Hot Spots

104337, Main Bank Transformer 1B Hot Spot

Calculations:

Calculation No. SQN- APS - 042, 480 V Turbine Building Common Board Load Coordination,

Short Circuit, Circuit Protection and Voltage Drop Analysis, Revision 4.

Calculation No. SQN-APS-041, 480 VAC Unit Board Load Coordination Study, Revision 4.

Work Orders:

6-771849-000, Check TE Accuracy, if unsatisfactory, Then Replace the TE

2-002298-000, Westinghouse Advisory Letter NSAL-02-3

03-012340-001, Replace degraded portion of 6900 V Diesel Generator 1A-A power cable

PP351A between Unit 1 Additional Equip. Bldg. And D/G exciter cubicle.

03-012340-002, Install section of new replacement cable PP351A from AEB-1 to MH-14 via

existing conduit.

Miscellaneous Documents:

Westinghouse Advisory Letter NSAL-03-9

ABB Power T&D- Sequoyah Nuclear Plant Final Report Main Generator Transformer Life

Assessment.

Drawings:

Drawing No. 1, 2-3591A28, Breaker Setting Sheet 480 V Unit Board 1A, Revision 5

Drawing No. 1, 2-3591A30, Breaker Setting Sheet 480 V Unit Board 1B, Revision 6.

Drawing No. 1, 2-3591A32, Breaker Setting Sheet 480 V Unit Board 2A, Revision 6.

Drawing No. 1, 2-3591A34, Breaker Setting Sheet 480 V Unit Board 2B, Revision 5

Drawing No. 1, 2-3591A36, Breaker Setting Sheet 480 V Turb. Building Common Board,

Revision 9 Drawing No. 1, 2-15E500-1, Key Diagram Station Auxiliary Power, Revision 25

Drawing No. 1, 2-15E500-3, Transformer Taps and Voltage Limits - Auxiliary Power System,

Revision 16.

Drawing No. 1-45N1504, Wiring Diagrams - Main Single Line 500 KV Switchyard, Revision 29

Attachment

A-9

Drawing No. 1-45W1541, Wiring Diagrams AC Schematic Unit 1 Generator & transformer

Circuits, Revision 14

Procedures:

TI-28, Rev. 198, Curve Book

PER Written Because of Inspection Finding

114743, Superseded ARP revision found in ACR

Section 1R19: Post Maintenance Testing

PER 115780, 2-FCV-74-28 Did Not Appear To Fully Open

2-SI-SXP-074-202.A, RHR Pump 2A-A Performance and Discharge Check Valve Test,

Revision 0

WO 06-780773-000, Calibrate 2-FCV-74-28 and Limit Switches

Section 1R20: Refueling and Outage Activities

0-GO-6, Power Reduction from 30& Reactor Power to Hot Standby, Revision 32

0-GO-7, Unit Shutdown From Hot Standby to Cold Shutdown, Revision 47

0-GO-15, Containment Closure Control, Revision 21

DVD Recording of U2C14 Core Load Verification

1,2-47W812-1, Flow Diagram Containment Spray System, Revision 42

Tagout Clearance 2-72-2406-RFO, Motor Operated Valve Maintenance on 2-FCV-72-21

0-GO-13, Reactor Coolant System Drain and Fill Operations, Revision 54

Sequoyah Nuclear Plant Unit 2 Cycle 15 Core Operating Limits Report

Section 1R22: Surveillance Testing

SPP-8.1 Conduct of Testing, Rev 4

Section 1EP6: Drill Evaluation

NEI 99-02 Rev 0, March 2000

Emergency Plan Implementing Procedure (EPIP) - 1, Emergency Plan Classification Matrix,

Rev 37

EPIP-3, Alert, Rev 29

EPIP-4, Site Area Emergency, Rev 29

EPIP-5, General Emergency, Rev 36

EPIP-6, Technical Support Center, Rev 41

EPIP-7, Operations Support Center, Rev 25

Section 2OS1: Access Control To Radiologically Significant Areas

Procedures, Instructions, Guidance Documents, and Operating Manuals

ANSI/ANS 3.1-1987, Selection, Qualification, and Training of Personnel for Nuclear Power

Plants

Tennessee Valley Authority (TVA), TVA Nuclear (TVAN), Standard Programs and

Attachment

A-10

Processes (SPP) - 3.1, Corrective Action Program, Rev. 11

Active Radiation Work Permits (RWPs) List, dated 12/11/2006

RP Personnel Identification by Craft Report, dated 12/14/2006

Task Qualification List (selected individuals), dated December 14, 2006

LHRA Key Control Log Sheets (several pages)

TVA, TVAN, TRN-20, Health Physics Technician Training, Rev. 13

High Radiation Areas at Sequoyah List, document not dated

SNP RP Organizational Chart (current and proposed changes), document not dated.

TVAN Radiation Protection Peer Team Challenge Update (MS Power Point presentation),

dated 12/13/2006

TVA, TVAN, SPP-5.2, ALARA Program, Rev. 3

RWP 06027010, Rev. 0, Routine Plant Maintenance-Lower Containment All Areas

RWP 06027035, Rev. 0, Routine Plant Maintenance-Inside Polar Crane All Areas

RWP 06027390, Rev. 1, Routine Plant Maintenance-Accumulator 1-4

RWP 06037020, Rev. 0, Inservice Inspection-Steam Generator Primary Side 1-4

RWP 06047141, Rev. 0, Refueling-U-2 Reactor Cavity

TVA, Sequoyah Nuclear Plant (SNP), Radiological Control Instruction (RCI)-01, Radiation

Protection Program

TVA, SNP, RCI-01, Training and Qualification of Health Physics Technicians-Radiation

Operations Technicians, effective date 02/24/05

TVA, SNP, RCI-14, Radiation Work Permit (RWP) Program, Rev. 37

TVA, SNP, RCI-15, Radiological Postings, Rev. 15

TVA, SNP, RCI-24, Control of Very High Radiation Areas, Rev. 7

TVA, SNP, RCI-28, Control of Locked High Radiation Areas, Rev. 5

TVA, SNP, RCI-29, Control of Radiation Protection Keys, Rev. 4

Records and Data Reviewed

SNS VSDS Survey Nos. 120506-2, 120606-8, 120506-15, 120606-10, 120606-7, 120706-2,

120106-10, 120606-6, and 120306-4

Air Sample Survey Nos. 120406018, 120506021, 120506024, 120506034, 120506037,

120506045, 120506048, 120506053, 120606020, 120706010,120406024, 120606028,

120506012, and 120606043

Corrective Action Program Documents

Nuclear Assurance (NA) - TVAN-Wide - Audit Report No. SSA0502 - Radiological Protection

and Control Audit, dated January 19, 2006

SQN-RP-05-001, Self-Assessment Report, dated 12/22/04

SQN-RP-05-003, Self-Assessment Report, dated 7/29/05

Problem Evaluation Report (PER) 82569, Presently U-1 Lower Containment Has a Ladder.

PER 115944, The Total Nozzle Dam Jumpers Dose Was Greater than the ALARA estimate

PER 101211, Posting and Control of Filter Cubicles...

PER 113913, Lock Box for Lifting Device Control

PER 109603, Radiation Posting

PER 109604, Radcon Use of Industry Information

PER 87610, Key Taken Home

PER 82027, High Radiation Readings on Valve

PER 82643, Unexpected Radiation Level Change

Attachment

A-11

PER 84532, VHRA Key Inventory

PER 99226, Locked High Radiation Door Locks Sticking

Section 4OA5: Other Activities - Operation of ISFSI

NEI 96-07, Guidelines for 10 CFR 72.48 Implementation, Appendix B

SPP-9.9, 10 CFR 72.48 Evaluations of Changes, Tests, and Experiments for Independent

Spent Fuel Storage Installation, Revision 1

Regulatory Guide 3.72 - Guidance for Implementation of 10 CFR 72.48, Changes, Tests and

Experiments

PER 95624, MPC-0011 Lid Did Not Fully Seat Due to Upper Fuel Spacers Not Vertical or

Plumb

10 CFR 48 Evaluation, Response to NRC IN 2003-16

10 CFR 48 Procedure Change Evaluation, Revision of NFTP-100, Fuel Selection for Dry MPC

Storage

10 CFR 48 Screening, Auxiliary Building Crane Truck Repairs

10 CFR 48 Screening, Auxiliary Building Crane Truck Replacements

10 CFR 48 Screening, Revision to Welding Procedures

10 CFR 48 Screening, Procedure Change to Fuel Handling Instruction FHI-14

10 CFR 48 Screening, Procedure Change to Fuel Handling Instruction FHI-3

Section 4OA5: Other Activities - TI 2515/150

Procedures

0-PI-DXX-068-100.R, Monitoring of Reactor Head Canopy Seal Welds For Leakage, Rev. 1

54-ISI-603-002, Automated Ultrasonic Examination of RPV Closure Head Penetrations

Containing Thermal Sleeves

54-ISI-604-001, Automated Ultrasonic Examination of Open Tube RPV Closure Head

Penetrations

54-ISI-605-02, Automated Ultrasonic Examination of RPV Closure Head Small Bore

Penetrations

54-ISI-240-44, Visible Solvent Removable Liquid Penetrant Examination Procedure

N-VT-17, Visual Examination for Leakage of PWR Reactor Head Penetrations, Rev. 4

SPP-9.7, Corrosion Control Program, Appendix D, Technical Requirements for the Boric Acid

Corrosion Control Program, Rev. 13

Records/Reports/Engineering Documents

Equipment Certification Records for the following NDE Equipment:

Blade Probes: S1035 NL, S5002 NL, and S5001 NL

Ultrasonic Transducers: 21GB-06001 and 2078-06001

Engineering Information Record 51-9027415-000, RPV Head Penetration Inspection Plan and

Coverage Assessment for Sequoyah Units 1 and 2

Calculation C-3217-00-02, Sequoyah 1 and 2 CRDM and Instrument Column Nozzle Stress

Analysis

Letter L44 030227 801, Response to issuance of NRC Order

Attachment

A-12

Corrective Action Documents

PER 115561, Evidence of leakage during canopy seal weld inspection

PER 116540*, EDY calculation not performed every outage

PER 116165*, Transducer frequencies documented incorrectly

  • Problem Evaluation Reports generated as a result of this inspection

Section 4OA5: Other Activities - TI 2515/166

Surveillance Instruction 2-SI-SIN-063-009-02, Containment Sump Inspection, dated 11/08/06

DCN 22023, Modify Containment Sump Screens as required by NEI Methodology, dated

11/22/06

Amendment to Facility Operating License No. 302, DPR-79, Revised Transport Analysis

Methodology for Containment Debris Transport, dated 11/07/06

TVA letter to NRC, Sequoyah Response to GL 2004-02. dated 9/01/05

AREVA document No. 51-9008500-003, Test Report for Sure-Flow strainer (Prototype)

Headloss Evaluation for Sequoyah 1 & 2 ECCS Containment Sumps, dated 7/26/06

AREVA document No. 51-9008506-001, Sequoyah Advanced Design Reactor Building Sump

Strainer Test Results Summary, Units 1 & 2, dated 1/31/06

GL 2004-02 Supplemental Response, Sequoyah Nuclear Plant Units 1 & 2, - NRC GL 2004-02,

Potential Impact of Debris Blockage on Emergency Recirculation during Design Basis

Accidents at PWRs (Draft dated 12/15/06)

Calculation ALION-CAL-TVA-2740-05, SQN Units 1 & 2 Containment Sump Debris

Accumulation and Head Loss, dated 6/28/05

Calculation TDI-6009-02, SFS Surface Area Flow Volume - TVA/Sequoyah 1 & 2, dated

9/21/06

MDQ0072980034, "CCP, SIP, CSP, and RHR Pump NPSH Evaluation", Rev 1, 11/19/2006

DCN # D22023, "Modify Containment Sump Screens as Required by NEI Methodology", Rev A,

11/22/2006

Calculation TDI-6009-004, "Module Debris Weight - TVA/Sequoyah - 1/2", Rev 2, 10/13/2006

Calculation PCI-5465-S01, "Structural Evaluation of Advanced Design Containment Building

Sump Strainers", Rev 0, 10/20/2006

Routine Work Order 06-774811-000, "Containment RHR Sump 48N919", Rev 5

FME Accountability Log, SPP 6.5.1

Section 4OA5: Other Activities - TI 2515/169

Procedures, Manuals, and Guidance Documents

NEI 99-02, Mitigating System Performance Index (MSPI) Basis Document, Revision 1

Selected System Status Reports

0-SI-SXV-063-266.0, ASME Section XI Valve Testing

1,2-SI-SXV-000-201.0, Full Stroking of Category A and B Valves During Operation

0-SI-SXV-074-266.0, ASME Section XI Valve Testing

1,2-SI-OPS-074-128.0, RHR Discharge Piping Vent

1-SI-SXP-074-074-201.B, RHR Pump 1B-B Performance Test

2-SI-SXP-074-074-201.B, RHR Pump 1B-B Performance Test

0-SI-SXV-000-221.0, Full Stroking of the Common ERCW and CCS Category A and B

Valves During Operation

Attachment

A-13

0-SI-OPS-067-682.Q, ERCW Non-Safety Related Flow Balance Valve Position Verification

0-SI-SXP-067-202.B, ERCW Traveling Screen Wash Pump B-B Performance Test

2-SI-OPS-070-32.A, Component Cooling Water Valves Position Verification Train A

Records and Data

Selected Control Room Logs, January 2004 through December 2006

EDG NRC Performance Indicators, 2002 - 2005

AFW NRC Performance Indicators, 2002 - 2005

HPSI NRC Performance Indicators, 2002 - 2005

RHR NRC Performance Indicators, 2002 - 2005

Consolidated Data Entry MSPI Derivation Reports Generated November 2006

MSPI Equipment Functional Failure Data Sheets

Maintenance Rule Unavailability Data Sheets, 2002-2006

Maintenance Rule Unreliability Data Sheets, 2002-2006

Corrective Action Program Documents

Selected Corrective Action Reports, 2005-2006

Attachment

LIST OF ACRONYMS

AFW auxiliary feedwater

ANSI American National Standards Institute

AOP abnormal operating procedures

ARC alternate repair criteria

ASME American Society of Mechanical Engineers

ATWS anticipated transient without scram

AUO auxiliary unit operator

BACC boric acid corrosion control

BMV bare metal visual

CCP cooling charging pump

CCPIT cooling charging pump injection tank

CFR Code of Federal Regulations

CR condition report

CRDM control rod drive mechanism

CVCS chemical volume control system

DCN design change notice

ECCS emergency core cooling system

ECT eddy current testing

EDY effective degradation years

ERCW essential raw cooling water

ETSS examination technique specifications sheet

FCV flow control valve

FE functional evaluation

FME foreign material exclusion

FOSAR foreign object search and recovery

HR high radiation

HUT holdup tank

INPO Institute of Nuclear power Operations

ISFSI independent spent fuel storage installation

ISI inservice inspection

LHRA locked high radiation area

MRP materials reliability program

MSPI mitigating systems performance index

NCV non-cited violation

NDE non-destructive examination

NRC U.S. Nuclear Regulatory Commission

ODSCC outer diameter stress corrosion cracking

OPDP operations department procedure

PAR publically available records

PER problem evaluation report

PER protective action recommendation

PORV power-operated relief valve

PWSCC primary water stress corrosion cracking

RCP reactor coolant pump

RCS reactor coolant system

RHR residual heat removal

RP radiation protection

Attachment

A-15

RPVH reactor pressure vessel head

RTP rated thermal power

RWP radiation work permit

RWST refueling water storage tank

SDP significance determination process

SER safety evaluation report

SG steam generator

SI safety injection

SI surveillance instructions

SSC structure, system, or component

TDAFP turbine driven auxiliary feedwater pump

TI temporary instruction

TS technical specification

TVA Tennessee Valley Authority

UFSAR updated final safety analysis report

UHI upper head injection

URI unresolved item

UT ultrasonic testing

WOs work orders

Attachment