PNO-II-07-002, NRC - Vogtle Unit 2 Notification of Unusual Event (Noue) Due to Reactor Coolant System (RCS) Leakage in Excess of 10 Gallons Per Minute (Gpm): Difference between revisions

From kanterella
Jump to navigation Jump to search
(Created page by program invented by StriderTol)
 
(Created page by program invented by StriderTol)
Line 14: Line 14:
| page count = 1
| page count = 1
}}
}}
{{#Wiki_filter:March 9, 2007PRELIMINARY NOTIFICATION OF EVENT OR UNUSUAL OCCURRENCE PNO-II-07-002This preliminary notification constitutes EARLY notice of events of possible safety or public interestsignificance. The information is as initially received without verification or evaluation, and is basically all that isknown by Region II staff (Atlanta, Georgia) on this date.FacilityLicensee Emergency ClassificationSouthern Nuclear CompanyXNotification of Unusual EventVogtle Unit 2Alert Waynesboro, GeorgiaSite Area Emergency Docket/License: 50-425/NPF-81General EmergencyNot Applicable
{{#Wiki_filter:March 9, 2007 PRELIMINARY NOTIFICATION OF EVENT OR UNUSUAL OCCURRENCE PNO-II-07-002 This preliminary notification constitutes EARLY notice of events of possible safety or public interest significance. The information is as initially received without verification or evaluation, and is basically all that is known by Region II staff (Atlanta, Georgia) on this date.
Facility                                                  Licensee Emergency Classification Southern Nuclear Company                                  X        Notification of Unusual Event Vogtle Unit 2                                                      Alert Waynesboro, Georgia                                                Site Area Emergency Docket/License: 50-425/NPF-81                                      General Emergency Not Applicable


==SUBJECT:==
==SUBJECT:==
VOGTLE UNIT 2 NOTIFICATION OF UNUSUAL EVENT (NOUE) DUE TO REACTORCOOLANT SYSTEM (RCS) LEAKAGE IN EXCESS OF 10 GALLONS PER MINUTE (GPM)At 2:23 p.m., EST on March 9, 2007, the licensee declared an NOUE for indication of Unit 2 RCS leakage inexcess of 10 gpm. Unit 2 had been shutdown for a scheduled refueling outage and an RCS draindownevolution was in progress. This declaration was based on control room operators detecting a mismatchbetween charging flow into the RCS and letdown flow out of the RCS of approximately 30 gpm. At the time ofthe event, the RCS was being cooled by the residual heat removal system, RCS temperature wasapproximately 90 degrees F, and the pressurizer was vented to the containment atmosphere.The NRC entered the Monitoring Mode at 3:08 p.m., and the Region II Incident Response Center was staffed.
VOGTLE UNIT 2 NOTIFICATION OF UNUSUAL EVENT (NOUE) DUE TO REACTOR COOLANT SYSTEM (RCS) LEAKAGE IN EXCESS OF 10 GALLONS PER MINUTE (GPM)
The licensee attributed the mismatch between charging and letdown to a gas pocket that formed in the reactorvessel head during the shutdown evolution. The gas pocket was released into the containment atmosphere,after the reactor vessel head vent was opened during the draindown evolution. The licensee stated that noleakage from the RCS was detected and that no unplanned radiological exposure to personnel occurred fromthe venting of the RCS. The unit will remain shutdown until the completion of the refueling outage. The resident inspectors we re in theplant and monitored the licensee's actions associated with this event. The licensee terminated the NOUE at 5:51 p.m., at which time the NRC exited the Monitoring Mode.
At 2:23 p.m., EST on March 9, 2007, the licensee declared an NOUE for indication of Unit 2 RCS leakage in excess of 10 gpm. Unit 2 had been shutdown for a scheduled refueling outage and an RCS draindown evolution was in progress. This declaration was based on control room operators detecting a mismatch between charging flow into the RCS and letdown flow out of the RCS of approximately 30 gpm. At the time of the event, the RCS was being cooled by the residual heat removal system, RCS temperature was approximately 90 degrees F, and the pressurizer was vented to the containment atmosphere.
The licensee has not received any inquiries from the media associated with this event and an NRC pressrelease is not planned.The information presented herein has been discussed with the licensee and is current as of 6:00 p.m., March 9, 2007.The State of Georgia has been notified of the event.Contact:Charles R. Ogle404-562-4605}}
The NRC entered the Monitoring Mode at 3:08 p.m., and the Region II Incident Response Center was staffed.
The licensee attributed the mismatch between charging and letdown to a gas pocket that formed in the reactor vessel head during the shutdown evolution. The gas pocket was released into the containment atmosphere, after the reactor vessel head vent was opened during the draindown evolution. The licensee stated that no leakage from the RCS was detected and that no unplanned radiological exposure to personnel occurred from the venting of the RCS.
The unit will remain shutdown until the completion of the refueling outage. The resident inspectors were in the plant and monitored the licensees actions associated with this event.
The licensee terminated the NOUE at 5:51 p.m., at which time the NRC exited the Monitoring Mode.
The licensee has not received any inquiries from the media associated with this event and an NRC press release is not planned.
The information presented herein has been discussed with the licensee and is current as of 6:00 p.m.,
March 9, 2007.
The State of Georgia has been notified of the event.
Contact:       Charles R. Ogle 404-562-4605}}


{{PNO-Nav|region=II}}
{{PNO-Nav|region=II}}

Revision as of 06:56, 23 November 2019

PNO-II-07-002 - NRC - Vogtle Unit 2 Notification of Unusual Event (Noue) Due to Reactor Coolant System (RCS) Leakage in Excess of 10 Gallons Per Minute (Gpm)
ML071200316
Person / Time
Site: Vogtle Southern Nuclear icon.png
Issue date: 03/09/2007
From: Ogle C
NRC/RGN-II
To:
C.R.Ogle, 404-562-4605
References
PNO-II-07-002
Download: ML071200316 (1)


March 9, 2007 PRELIMINARY NOTIFICATION OF EVENT OR UNUSUAL OCCURRENCE PNO-II-07-002 This preliminary notification constitutes EARLY notice of events of possible safety or public interest significance. The information is as initially received without verification or evaluation, and is basically all that is known by Region II staff (Atlanta, Georgia) on this date.

Facility Licensee Emergency Classification Southern Nuclear Company X Notification of Unusual Event Vogtle Unit 2 Alert Waynesboro, Georgia Site Area Emergency Docket/License: 50-425/NPF-81 General Emergency Not Applicable

SUBJECT:

VOGTLE UNIT 2 NOTIFICATION OF UNUSUAL EVENT (NOUE) DUE TO REACTOR COOLANT SYSTEM (RCS) LEAKAGE IN EXCESS OF 10 GALLONS PER MINUTE (GPM)

At 2:23 p.m., EST on March 9, 2007, the licensee declared an NOUE for indication of Unit 2 RCS leakage in excess of 10 gpm. Unit 2 had been shutdown for a scheduled refueling outage and an RCS draindown evolution was in progress. This declaration was based on control room operators detecting a mismatch between charging flow into the RCS and letdown flow out of the RCS of approximately 30 gpm. At the time of the event, the RCS was being cooled by the residual heat removal system, RCS temperature was approximately 90 degrees F, and the pressurizer was vented to the containment atmosphere.

The NRC entered the Monitoring Mode at 3:08 p.m., and the Region II Incident Response Center was staffed.

The licensee attributed the mismatch between charging and letdown to a gas pocket that formed in the reactor vessel head during the shutdown evolution. The gas pocket was released into the containment atmosphere, after the reactor vessel head vent was opened during the draindown evolution. The licensee stated that no leakage from the RCS was detected and that no unplanned radiological exposure to personnel occurred from the venting of the RCS.

The unit will remain shutdown until the completion of the refueling outage. The resident inspectors were in the plant and monitored the licensees actions associated with this event.

The licensee terminated the NOUE at 5:51 p.m., at which time the NRC exited the Monitoring Mode.

The licensee has not received any inquiries from the media associated with this event and an NRC press release is not planned.

The information presented herein has been discussed with the licensee and is current as of 6:00 p.m.,

March 9, 2007.

The State of Georgia has been notified of the event.

Contact: Charles R. Ogle 404-562-4605