ML080770308: Difference between revisions

From kanterella
Jump to navigation Jump to search
(Created page by program invented by StriderTol)
(Created page by program invented by StriderTol)
Line 17: Line 17:


=Text=
=Text=
{{#Wiki_filter:UNITED STATES NUCLEAR REGULATORY COMMISSION  
{{#Wiki_filter:UNITED STATES
REGION I 475 ALLENDALE ROAD KING OF PRUSSIA, PA 19406-1415  
                          NUCLEAR REGULATORY COMMISSION
March 17, 2008  
                                              REGION I
 
                                        475 ALLENDALE ROAD
                                  KING OF PRUSSIA, PA 19406-1415
                                          March 17, 2008
Mr. Britt T. McKinney
Mr. Britt T. McKinney Senior Vice President and Chief Nuclear Officer  
Senior Vice President and Chief Nuclear Officer
PPL Susquehanna, LLC  
PPL Susquehanna, LLC
769 Salem Blvd. - NUCSB3
Berwick, PA 18603-0467
SUBJECT:        SUSQUEHANNA STEAM ELECTRIC STATION, UNITS 1 AND 2
                PROBLEM IDENTIFICATION AND RESOLUTION INSPECTION
                INSPECTION REPORTS NOS. 05000387/2008006; 05000388/2008006
Dear Mr. McKinney:
On February 1, 2008, the US Nuclear Regulatory Commission (NRC) completed a team
inspection at the Susquehanna Steam Electric Station. The enclosed inspection report
documents the inspection results, which were discussed on February 1, 2008, with you and
members of your staff.
This inspection was an examination of activities conducted under your license as they relate to
the identification and resolution of problems, and compliance with the Commission=s rules and
regulations and the conditions of your license. Within these areas, the inspection involved
examination of selected procedures and representative records, observations of activities, and
interviews with personnel.
On the basis of the sample selected for review, the team concluded that the implementation of
the corrective action program (CAP) was adequate in that personnel identified issues at a low
threshold; generally screened and prioritized issues in a timely manner; evaluated the issues
commensurate with their safety significance; and implemented corrective actions in a timely
manner commensurate with the safety significance.
The team identified four findings of very low safety significance (Green). These findings were
determined to involve violations of regulatory requirements. However, because each of the
violations was of very low safety significance (Green) and because they were entered into your
corrective action program, the NRC is treating these as Non-Cited Violations (NCVs), in
accordance with Section VI.A.1 of the NRC=s Enforcement Policy. If you contest any NCV in
this report, you should provide a response within 30 days of the date of this inspection report,
with the basis for your denial, to the U.S. Nuclear Regulatory Commission, ATTN: Document
Control Desk, Washington DC, 20555-0001, with copies to the Regional Administrator, Region I;


769 Salem Blvd. - NUCSB3
B. McKinney                                      2
the Director, Office of Enforcement, U.S. Nuclear Regulatory Commission, Washington, DC,
20555-0001; and the NRC Resident Inspector at the Susquehanna facility.
In accordance with 10 CFR 2.390 of the NRC=s ARules of Practice,@ a copy of this letter and its
enclosure, and your response (if any), will be available electronically for public inspection in the
NRC Public Document Room or from the Publicly Available Records (PARS) component of the
NRC=s document system (ADAMS). ADAMS is accessible from the NRC Web site at
http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room).
                                              Sincerely,
                                              /RA/
                                              Mel Gray, Chief
                                              Technical Support & Assessment Branch
                                              Division of Reactor Projects
Docket Nos. 50-387, 50-388
License Nos. NPF-14; NPF-22
Enclosure:      Inspection Report Nos. 05000387/2008006; 05000388/2008006
                  w/ Attachment: Supplemental Information
cc w/encl:
C. Gannon, Vice President, Nuclear Operations
R. Paley, General Manager, Plant Support
R. Pagodin, General Manager, Nuclear Engineering
R. Sgarro, Manager, Nuclear Regulatory Affairs
Supervisor, Nuclear Regulatory Affairs
M. Crowthers, Supervising Engineer, Nuclear Regulatory Affairs
R. Peal, Mgr, Training, Susquehanna
Manager, Quality Assurance
J. Scopelliti, Community Relations Manager, Susquehanna
B. Snapp, Esq., Associate General Counsel, PPL Services Corporation
Supervisor - Document Control Services
R. Osborne, Allegheny Electric Cooperative, Inc.
D. Allard, Dir, PA Dept of Environmental Protection
Board of Supervisors, Salem Township
J. Johnsrud, National Energy Committee, Sierra Club
E. Epstein, TMI-Alert (TMIA)
J. Powers, Dir, PA Office of Homeland Security
R. French, Dir, PA Emergency Management Agency


Berwick, PA 18603-0467  
                                          1
                  U.S. NUCLEAR REGULATORY COMMISSION
                                      REGION I
Docket No:  50-387, 50-388
License No:  NPF-14, NPF-22
Report No:  05000387/2008006, 05000388/2008006
Licensee:    PPL Susquehanna, LLC
Facility:    Susquehanna Steam Electric Station, Units 1 and 2
Location:    769 Salem Boulevard - NUCSB3
            Berwick, PA 18603-0467
Dates:      January 14 - February 1, 2008
Team Leader: B. Norris, Senior Project Engineer, Division of Reactor Projects
Inspectors:  F. Arner, Senior Reactor Inspector, Division of Reactor Safety
            R. Fuhrmeister, Senior Project Engineer, Division of Reactor Projects
            G. Ottenberg, Resident Inspector, Division of Reactor Projects
            J. Bream, Reactor Engineer, Division of Reactor Projects
            R. McKinley, Operations Examiner, Division of Reactor Safety
Approved by: Mel Gray, Chief
            Technical Support & Assessment Branch
            Division of Reactor Projects
                                                                                  Enclosure


SUBJECT: SUSQUEHANNA STEAM ELECTRIC STATION, UNITS 1 AND 2 PROBLEM IDENTIFICATION AND RESOLUTION INSPECTION
                                                  2
INSPECTION REPORTS NOS. 05000387/2008006; 05000388/2008006
                                    SUMMARY OF FINDINGS
IR 05000387/2008-006, 05000388/2008-006; 01/14/2008 - 02/01/2008; Susquehanna Steam
Dear Mr. McKinney:
Electric Station; Biennial Baseline Inspection of the Identification and Resolution of Problems;
On February 1, 2008, the US Nuclear Regulatory Commission (NRC) completed a team
Corrective Action Program, Simulator Fidelity, and Procedure Quality.
inspection at the Susquehanna Steam Electric Station.  The enclosed inspection report
This team inspection was performed by five NRC regional inspectors and one resident
documents the inspection results, which were discussed on February 1, 2008, with you and
inspector. Four findings of very low safety significance (Green) were identified during this
members of your staff.
inspection and determined to be Non-Cited Violations (NCVs). The significance of most findings
 
is indicated by their color (Green, White, Yellow, Red) using NRC Inspection Manual Chapter
This inspection was an examination of activities conducted under your license as they relate to the identification and resolution of problems, and compliance with the Commission
(IMC) 0609, ASignificance Determination Process@ (SDP). The NRC=s program for overseeing
=s rules and regulations and the conditions of your license.  Within these areas, the inspection involved examination of selected procedures and representative records, observations of activities, and interviews with personnel.
the safe operation of commercial nuclear power reactors is described in NUREG-1649, AReactor
 
Oversight Process,@ Revision 4, dated December 2006.
On the basis of the sample selected for review, the team concluded that the implementation of
the corrective action program (CAP) was adequate in that personnel identified issues at a low threshold; generally screened and prioritized issues in a timely manner; evaluated the issues commensurate with their safety significance; and implemented corrective actions in a timely manner commensurate with the safety significance. 
 
The team identified four findings of very low safety significance (Green).  These findings were determined to involve violations of regulatory requirements.  However, because each of the violations was of very low safety significance (Green) and because they were entered into your corrective action program, the NRC is treating these as Non-Cited Violations (NCVs), in accordance with Section VI.A.1 of the NRC
=s Enforcement Policy.  If you contest any NCV in this report, you should provide a response within 30 days of the date of this inspection report,
with the basis for your denial, to the U.S. Nuclear Regulatory Commission, ATTN:  Document
Control Desk, Washington DC, 20555-0001, with copies to the Regional Administrator, Region I; 
B. McKinney
2the Director, Office of Enforcement, U.S. Nuclear Regulatory Commission, Washington, DC, 20555-0001; and the NRC Resident Inspector at the Susquehanna facility.
In accordance with 10 CFR 2.390 of the NRC
=s A Rules of Practice,@ a copy of this letter and its enclosure, and your response (if any), will be available electronically for public inspection in the NRC Public Document Room or from the Publicly Available Records (PARS) component of the
NRC=s document system (ADAMS).  ADAMS is accessible from the NRC Web site at http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room).
Sincerely,  /RA/  Mel Gray, Chief Technical Support & Assessment Branch
Division of Reactor Projects
Docket Nos.  50-387, 50-388
License Nos.  NPF-14; NPF-22
Enclosure:  Inspection Report Nos. 05000387/2008006; 05000388/2008006    w/ Attachment:  Supplemental Information
cc w/encl: 
C. Gannon, Vice President, Nuclear Operations 
R. Paley, General Manager, Plant Support R. Pagodin, General Manager, Nuclear Engineering 
 
R. Sgarro, Manager, Nuclear Regulatory Affairs
 
Supervisor, Nuclear Regulatory Affairs
 
M. Crowthers, Supervising Engineer, Nuclear Regulatory Affairs R. Peal, Mgr, Training, Susquehanna
Manager, Quality Assurance
J. Scopelliti, Community Relations Manager, Susquehanna 
B. Snapp, Esq., Associate General Counsel, PPL Services Corporation
 
Supervisor - Document Control Services
R. Osborne, Allegheny Electric Cooperative, Inc. D. Allard, Dir, PA Dept of Environmental Protection 
Board of Supervisors, Salem Township
J. Johnsrud, National Energy Committee, Sierra Club
E. Epstein, TMI-Alert (TMIA)
 
J. Powers, Dir, PA Office of Homeland Security R. French, Dir, PA Emergency Management Agency
 
  Enclosure
1 U.S. NUCLEAR REGULATORY COMMISSION
REGION I
  Docket No: 50-387, 50-388
License No: NPF-14, NPF-22
 
  Report No: 05000387/2008006, 05000388/2008006
 
Licensee: PPL Susquehanna, LLC
 
  Facility: Susquehanna Steam Electric Station, Units 1 and 2  
 
Location: 769 Salem Boulevard - NUCSB3  Berwick, PA  18603-0467
Dates: January 14 - February 1, 2008
 
  Team Leader: B. Norris, Senior Project Engineer, Division of Reactor Projects
 
Inspectors: F. Arner, Senior Reactor Inspector, Division of Reactor Safety
R. Fuhrmeister, Senior Project Engineer, Division of Reactor Projects  G. Ottenberg, Resident Inspector, Division of Reactor Projects  J. Bream, Reactor Engineer, Division of Reactor Projects
R. McKinley, Operations Examiner, Division of Reactor Safety
 
Approved by: Mel Gray, Chief  Technical Support & Assessment Branch
Division of Reactor Projects
 
 
  Enclosure
2SUMMARY OF FINDINGS
  IR 05000387/2008-006, 05000388/2008-006; 01/14/2008 - 02/01/2008; Susquehanna Steam Electric Station; Biennial Baseline Inspection of the Identification and Resolution of Problems; Corrective Action Program, Simulator Fidelity, and Procedure Quality.  
 
This team inspection was performed by five NRC regional inspectors and one resident  
inspector. Four findings of very low safety significance (Green) were identified during this inspection and determined to be Non-Cited Violations (NCVs). The significance of most findings is indicated by their color (Green, White, Yellow, Red) using NRC Inspection Manual Chapter (IMC) 0609, ASignificance Determination Process
@ (SDP). The NRC
=s program for overseeing  
the safe operation of commercial nuclear power reactors is described in NUREG-1649, A Reactor Oversight Process,@ Revision 4, dated December 2006.  
Identification and Resolution of Problems
Identification and Resolution of Problems
 
The team concluded that the implementation of the corrective action program (CAP) at
The team concluded that the implementation of the corrective action program (CAP) at  
Susquehanna was adequate in that personnel identified issues at a low threshold and used a
Susquehanna was adequate in that personnel identified issues at a low threshold and used a single entry-point system to document the problems by the initiation of an Action Request (AR). About 20 percent of the ARs were considered to be conditions adverse to quality (CAQ) and  
single entry-point system to document the problems by the initiation of an Action Request (AR).
sub-classified as a Condition Report (CR). However, the team identified several ARs that  
About 20 percent of the ARs were considered to be conditions adverse to quality (CAQ) and
should have been classified as CAQs; as a result, CRs were not written and corrective actions  
sub-classified as a Condition Report (CR). However, the team identified several ARs that
were not timely. The team identified two findings of very low significance related to the AR process that had current performance cross-cutting aspects in problem identification because the issues were not categorized commensurate with their safety significance. Notwithstanding  
should have been classified as CAQs; as a result, CRs were not written and corrective actions
these two findings, the team concluded that in general Susquehanna personnel screened and  
were not timely. The team identified two findings of very low significance related to the AR
prioritized CRs in a timely manner using established criteria.  
process that had current performance cross-cutting aspects in problem identification because
the issues were not categorized commensurate with their safety significance. Notwithstanding
these two findings, the team concluded that in general Susquehanna personnel screened and
prioritized CRs in a timely manner using established criteria.
The team also concluded that Susquehanna personnel properly evaluated the issues
commensurate with their safety significance; and generally implemented corrective actions in a
timely manner, commensurate with the safety significance. The team noted that Susquehanna
reviewed and applied industry operating experience lessons learned. Audits and self-
assessments added value to the corrective action process. On the basis of interviews
conducted during the inspection, workers at the site expressed freedom to enter safety
concerns into the CAP.
                                                                                          Enclosure


   
                                                    3
The team also concluded that Susquehanna personnel properly evaluated the issues commensurate with their safety significance; and generally implemented corrective actions in a timely manner, commensurate with the safety significance. The team noted that Susquehanna  
a. NRC Identified and Self-Revealing Findings
reviewed and applied industry operating experience lessons learned. Audits and self-
  Cornerstone: Mitigating Systems
assessments added value to the corrective action process. On the basis of interviews
  C Green: The NRC identified a Non-Cited Violation of 10 CFR 50, Appendix B, Criterion V,
conducted during the inspection, workers at the site expressed freedom to enter safety concerns into the CAP.  
      Instructions, Procedures, and Drawings, because, in the 1990s, Susquehanna failed to
 
      adequately evaluate a deviation from the Boiling Water Reactor Owners Group
  Enclosure
      Emergency Procedure Guidelines / Severe Accident Guidelines (BWROG EPG/SAG),
3a. NRC Identified and Self-Revealing Findings
      which resulted in one of the emergency operating procedures (EOPs) being inadequate.
  Cornerstone: Mitigating Systems
      Specifically, Caution #1 in the BWROG EPG/SAG warned the operators that reactor
  Green: The NRC identified a Non-Cited Violation of 10 CFR 50, Appendix B, Criterion V, "Instructions, Procedures, and Drawings," because, in the 1990s, Susquehanna failed to  
      pressure vessel (RPV) level instrumentation may be unreliable if the drywell
      temperatures exceeded RPV saturation temperature. The purpose of the Caution was
      to give the operators a chance to evaluate the validity of the RPV level instrumentation
      to avoid premature entry into the RPV flooding contingency procedure. Susquehanna
      did not adequately evaluate the deviation, and the Susquehanna EOPs did not use a
      Caution statement; but instead, changed the caution to a procedural step, which directed
      the operators to transition directly to the RPV flooding procedure.
      The performance deficiency is more than minor because it is associated with the
      Procedure Quality attribute of the Mitigating Systems cornerstone and affects the
      objective to ensure the availability, reliability, and capability of systems that respond to
      initiating events to prevent undesirable consequences. Specifically, the EOP could have
      directed entry into the RPV flooding procedure unnecessarily which would have
      restricted the use of suppression pool cooling and required other actions that would have
      complicated the operators response to the event. The finding was determined to be of
      very low safety significance because it was not a design deficiency, did not result in an
      actual loss of safety function, and did not screen as potentially risk significant due to
      external initiating events. (Section 4OA2.a.3 (a))
  C Green: The NRC identified a Non-Cited Violation of 10 CFR 50, Appendix B, Criterion
      XVI, Corrective Action, for the failure to identify that an inconsistency between the
      procedures and the design basis for suppression pool (SP) cooling was a condition
      adverse to quality (CAQ), which resulted in corrective actions not being taken in a timely
      manner. Specifically, in January 2006, a Condition Report (CR) identified an
      inconsistency between an assumption in the Final Safety Analysis Report (FSAR) for the
      design basis accident and the emergency operating procedures (EOPs) regarding the
      timing for the implementation of SP cooling. At the time of the inspection, the
      inconsistency had not been resolved because Susquehanna did not recognize that it
      impacted current plant operations. This performance deficiency has a cross-cutting
      aspect in the area of Problem Identification and Resolution, Corrective Action Program,
      because Susquehanna did not identify that the inconsistency documented in the CR
      should have been categorized as a CAQ, commensurate with its safety significance.
      [P.1(a)]
      The performance deficiency is more than minor because it is associated with the Design
      Control attribute of Mitigating Systems and affects the cornerstone objective to ensure
      the availability, reliability, and capability of systems that respond to initiating events to
                                                                                              Enclosure


adequately evaluate a deviation from the Boiling Water Reactor Owner's Group
                                              4
Emergency Procedure Guidelines / Severe
  prevent undesirable consequences. Specifically, the EOPs provided direction that,
Accident Guidelines (BWROG EPG/SAG), which resulted in one of the emergency operating procedures (EOPs) being inadequate. Specifically, Caution #1 in the BWROG EPG/SAG warned the operators that reactor
  under some accident conditions, would affect the availability and/or capability of the SP
  cooling system to perform its safety function. The finding screened out as having very
  low safety significance because it was not a design deficiency, did not result in an actual
  loss of safety function, and did not screen as potentially risk significant due to external
  initiating events. (Section 4OA2.a.3 (b))
C Green: The NRC identified a Non-Cited Violation of 10 CFR 55.46(c)(1), Plant
  Referenced Simulators, because the Susquehanna simulator did not accurately model
  reactor pressure vessel (RPV) level instrumentation following a design basis accident
  loss of coolant accident (DBA LOCA). Specifically, an analysis performed in 1994 to
  determine if the observed simulator response during a large break LOCA was consistent
  with the expected plant response, was based on an overly conservative assumption that
  the drywell would experience superheated conditions, which would cause RPV water
  level instrumentation reference leg flashing and a subsequent loss of all RPV level
  indication. The expected plant response, as stated in the analysis, was incorrect; in that
  a LOCA would not always cause a loss of all RPV level instruments. As a result, the
  simulator modeling was incorrect.
  The performance deficiency is more than minor because it is associated with the Human
  Performance attribute of Mitigating Systems and affects the cornerstone objective to
  ensure the availability, reliability, and capability of systems that respond to initiating
  events to prevent undesirable consequences. Specifically, the modeling of the
  Susquehanna simulator introduced negative operator training that could affect the ability
  of the operators (a mitigating system) to take the appropriate actions during an actual
  event. The finding was determined to be of very low safety significance because it is not
  related to operator performance during requalification, it is related to simulator fidelity,
  and it could have a negative impact on operator actions. (Section 4OA2.a.3 (c))
C Green: The NRC identified a Non-Cited Violation of 10 CFR 50, Appendix B, Criterion
  XVI, Corrective Action, for the failure to identify that a setpoint error in the operating
  procedures for safety-related systems was a condition adverse to quality (CAQ),
  resulting in the procedures not being corrected in a timely manner. The setpoint for the
  low pressure injection permissive interlock in the RHR and CS systems had been
  changed in 1999 as part of a modification. However, the setpoint was not changed in
  the system operating procedures and operator aids. When this issue was identified by
  Susquehanna staff in 2006, the setpoint error in the procedure was not screened as a
  CAQ, which resulted in the procedures not being revised for 17 months after the issue
  was identified in an Action Report. This performance deficiency has a cross-cutting
  aspect in the area of Problem Identification and Resolution, Corrective Action Program,
  because Susquehanna did not identify that a setpoint error in operating procedures for
  safety-related systems was a CAQ, commensurate with its safety significance. [P.1(a)]
  The performance deficiency is more than minor because it is associated with the
  Procedure Quality attribute of Mitigating Systems and affects the cornerstone objective
  to ensure the availability, reliability, and capability of systems that respond to initiating
  events to prevent undesirable consequences. Specifically, the incorrect setpoint
                                                                                          Enclosure


pressure vessel (RPV) level instrumentation may be unreliable if the drywell
                                                  5
temperatures exceeded RPV saturation temperature.  The purpose of the Caution was
      reference in the procedure impacted the reliability of operator response to the event in
to give the operators a chance to evaluate the validity of the RPV level instrumentation
      that it could delay operator actions or result in misoperation of equipment. The finding
to avoid premature entry into the RPV flooding contingency procedure.  Susquehanna did not adequately evaluate the deviation, and the Susquehanna EOPs did not use a Caution statement; but instead, changed the caution to a procedural step, which directed
      screened out as having very low safety significance because it was not a design
the operators to transition directly to the RPV flooding procedure.
      deficiency, did not result in an actual loss of safety function, and did not screen as
The performance deficiency is more than minor because it is associated with the Procedure Quality attribute of the Mitigating Systems cornerstone and affects the objective to ensure the availability, reliability, and capability of systems that respond to
      potentially risk significant due to external initiating events. (Section 4OA2.a.3 (e))
initiating events to prevent undesirable consequences.  Specifically, the EOP could have
b. Licensee-Identified Violations
directed entry into the RPV flooding procedure unnecessarily which would have
  None.
restricted the use of suppression pool cooling and required other actions that would have
                                                                                            Enclosure
complicated the operators' response to the event. The finding was determined to be of very low safety significance because it was not a design deficiency, did not result in an actual loss of safety function, and did not screen as potentially risk significant due to  
external initiating events. (Section 4OA2.a.3 (a))  


  Green:  The NRC identified a Non-Cited Violation of 10 CFR 50, Appendix B, Criterion XVI, "Corrective Action," for the failure to identify that an inconsistency between the procedures and the design basis for suppression pool (SP) cooling was a condition
                                              6
adverse to quality (CAQ), which resulted in corrective actions not being taken in a timely
                                      REPORT DETAILS
manner.  Specifically, in January 2006, a Condition Report (CR) identified an
4.   OTHER ACTIVITIES (OA)
inconsistency between an assumption in the Final Safety Analysis Report (FSAR) for the
4OA2 Problem Identification and Resolution (PI&R) (Biennial - IP 71152B)
design basis accident and the emergency operating procedures (EOPs) regarding the timing for the implementation of SP cooling.  At the time of the inspection, the inconsistency had not been resolved because Susquehanna did not recognize that it
  a. Assessment of the Corrective Action Program
impacted current plant operations.  This performance deficiency has a cross-cutting
  1. Inspection Scope
aspect in the area of Problem Identification and Resolution, Corrective Action Program,
    The inspection team reviewed the procedures describing the corrective action program
because Susquehanna did not identify that the inconsistency documented in the CR should have been categorized as a CAQ, commensurate with its safety significance. 
    (CAP) at the Susquehanna Steam Electric Station. Susquehanna used a single-point
[P.1(a)]
    entry system and identified problems by the initiation of an Action Request (AR). The
    AR would then be sub-classified depending on the information provided; for example, as
The performance deficiency is more than minor because it is associated with the Design
    WO for a maintenance Work Order, as CPG for assignment to the Central Procedure
Control attribute of Mitigating Systems and affects the cornerstone objective to ensure the availability, reliability, and capability of systems that respond to initiating events to 
    Group, or as CR for a Condition Report. ARs were sub-classified as CRs for conditions
  Enclosure
    adverse to quality (CAQ), such as plant equipment deficiencies, industrial or radiological
4prevent undesirable consequences.  Specifical
    safety concerns, or other significant issues. The CRs were subsequently screened for
ly, the EOPs provided direction that, under some accident conditions, would affect the availability and/or capability of the SP
    operability and reportability, categorized by significance (1 to 3), assigned a level of
cooling system to perform its safety function.  The finding screened out as having very low safety significance because it was not a design deficiency, did not result in an actual loss of safety function, and did not screen as potentially risk significant due to external
    evaluation, and issued for resolution.
initiating events.  (Section 4OA2.a.3 (b))
    The team reviewed CRs selected across the seven cornerstones of safety in the NRC=s
    Reactor Oversight Process (ROP) to determine if problems were being properly
Green:  The NRC identified a Non-Cited Violation of 10 CFR 55.46(c)(1), "Plant Referenced Simulators," because the Susquehanna simulator did not accurately model reactor pressure vessel (RPV) level instrumentation following a design basis accident
    identified, characterized, and entered into the CAP for evaluation and resolution. The
loss of coolant accident (DBA LOCA).  Specifically, an analysis performed in 1994 to
    team selected items from the maintenance, operations, engineering, emergency
determine if the observed simulator response during a large break LOCA was consistent
    preparedness, physical security, radiation safety, training, and oversight programs to
with the expected plant response, was based on an overly conservative assumption that
    ensure that Susquehanna was appropriately considering problems identified in each
the drywell would experience superheated conditions, which would cause RPV water level instrumentation reference leg flashing and a subsequent loss of all RPV level indication.  The expected plant response, as stated in the analysis, was incorrect; in that
    functional area. The team used this information to select a risk-informed sample of CRs
a LOCA would not always cause a loss of all RPV level instruments.  As a result, the
    that had been issued since the last NRC PI&R inspection, which was conducted in
simulator modeling was incorrect.
    February 2006.
 
    The team selected ARs from other sub-classifications, to determine if Susquehanna had
The performance deficiency is more than minor because it is associated with the Human Performance attribute of Mitigating Systems and affects the cornerstone objective to
    appropriately classified these items as not needing to be a CR. The team also reviewed
ensure the availability, reliability, and capability of systems that respond to initiating
    operator log entries, control room deficiency lists, operator work-around lists, operability
events to prevent undesirable consequences.  Specifically, the modeling of the
    determinations, engineering system health reports, completed surveillance tests, and
Susquehanna simulator introduced negative operator training that could affect the ability
    current temporary configuration change packages. In addition, the team interviewed
of the operators (a mitigating system) to take the appropriate actions during an actual event.  The finding was determined to be of very low safety significance because it is not related to operator performance during requalification, it is related to simulator fidelity,
    plant staff and management to determine their understanding of and involvement with
and it could have a negative impact on operator actions.    (Section 4OA2.a.3 (c))
    the CAP at Susquehanna. The CRs, and other documents reviewed, and the key
 
    personnel contacted, are listed in the Attachment to this report.
  Green:  The NRC identified a Non-Cited Violation of 10 CFR 50, Appendix B, Criterion XVI, "Corrective Action," for the failure to identify that a setpoint error in the operating procedures for safety-related systems was a condition adverse to quality (CAQ), resulting in the procedures not being corrected in a timely manner.  The setpoint for the
    The team considered risk insights from the NRC=s and Susquehanna=s risk analyses to
low pressure injection permissive interlock in the RHR and CS systems had been
    focus the sample selection and plant tours on risk-significant components. The team
changed in 1999 as part of a modification.  However, the setpoint was not changed in
    determined that the five highest risk-significant systems at Susquehanna were
the system operating procedures and operator aids.  When this issue was identified by Susquehanna staff in 2006, the setpoint error in the procedure was not screened as a CAQ, which resulted in the procedures not being revised for 17 months after the issue
    emergency service water, emergency diesel generators, residual heat removal service
was identified in an Action Report.  This performance deficiency has a cross-cutting
    water, station black-out diesel generator, and reactor core isolation cooling. For the
aspect in the area of Problem Identification and Resolution, Corrective Action Program,
    risk-significant systems, the team reviewed a sample of the applicable system health
because Susquehanna did not identify that a setpoint error in operating procedures for safety-related systems was a CAQ, commensurate with its safety significance.  [P.1(a)]
                                                                                          Enclosure
The performance deficiency is more than minor because it is associated with the
Procedure Quality attribute of Mitigating Systems and affects the cornerstone objective
to ensure the availability, reliability, and capability of systems that respond to initiating events to prevent undesirable consequences.  Specifically, the incorrect setpoint 
  Enclosure
5reference in the procedure impacted the reliability of operator response to the event in that it could delay operator actions or result in misoperation of equipment.  The finding
screened out as having very low safety significance because it was not a design deficiency, did not result in an actual loss of safety function, and did not screen as potentially risk significant due to external initiating events.  (Section 4OA2.a.3 (e))
b. Licensee-Identified Violations
  None. 
  Enclosure
6REPORT DETAILS
 
4. OTHER ACTIVITIES (OA)
  4OA2 Problem Identification and Resolution (PI&R) (Biennial - IP 71152B)
 
  a. Assessment of the Corrective Action Program
    1. Inspection Scope
  The inspection team reviewed the procedures describing the corrective action program  
(CAP) at the Susquehanna Steam Electric Station. Susquehanna used a single-point  
 
entry system and identified problems by the initiation of an Action Request (AR). The AR would then be sub-classified depending on the information provided; for example, as WO for a maintenance Work Order, as CPG for assignment to the Central Procedure Group, or as CR for a Condition Report. ARs were sub-classified as CRs for conditions  
adverse to quality (CAQ), such as plant equipment deficiencies, industrial or radiological  
safety concerns, or other significant issues. The CRs were subsequently screened for operability and reportability, categorized by significance (1 to 3), assigned a level of evaluation, and issued for resolution.  
The team reviewed CRs selected across the seven cornerstones of safety in the NRC
=s Reactor Oversight Process (ROP) to determine if problems were being properly  
identified, characterized, and entered into the CAP for evaluation and resolution. The  
team selected items from the maintenance, operations, engineering, emergency  
preparedness, physical security, radiation safety, training, and oversight programs to  
ensure that Susquehanna was appropriately considering problems identified in each  
functional area. The team used this information to select a risk-informed sample of CRs that had been issued since the last NRC PI&R inspection, which was conducted in  
February 2006.  
The team selected ARs from other sub-classifications, to determine if Susquehanna had  
appropriately classified these items as not needing to be a CR. The team also reviewed operator log entries, control room deficiency lists, operator work-around lists, operability determinations, engineering system health reports, completed surveillance tests, and  
current temporary configuration change packages. In addition, the team interviewed  
plant staff and management to determine their understanding of and involvement with  
 
the CAP at Susquehanna. The CRs
, and other documents reviewed, and the key personnel contacted, are listed in the Attachment to this report.  
The team considered risk insights from the NRC
=s and Susquehanna
=s risk analyses to focus the sample selection and plant tours on risk-significant components. The team determined that the five highest risk-significant systems at Susquehanna were emergency service water, emergency diesel generators, residual heat removal service  
water, station black-out diesel generator, and reactor core isolation cooling. For the  
risk-significant systems, the team reviewed a sample of the applicable system health
  Enclosure  
7reports, work requests and engineering documents, plant log entries, and results from surveillance tests and maintenance tasks.
 
The team reviewed CRs to assess whether Susquehanna adequately evaluated and prioritized the identified problems.  The CRs reviewed encompassed the full range of
Susquehanna
=s causal evaluations, including root cause analyses (RCA - to determine the cause and prevent recurrence), apparent cause evaluations (ACE - to obtain a basic
understanding of the cause), and evaluations (to determine if a problem exists).  The
review included the appropriateness of the assigned significance, the scope and depth
of the causal analysis, and the timeliness of the resolutions.  For significant conditions
adverse to quality, the team reviewed the effectiveness of the corrective actions to
prevent recurrence.  The team observed meetings of the CR Screening Team - in which Susquehanna personnel reviewed new CRs for prioritization, and evaluated preliminary corrective action assignments, analyses, and plans.  The team also attended meetings of the Corrective Action Review Board (CARB) - where senior managers reviewed selected evaluations, effectiveness reviews, and extension requests. 
 
The team reviewed equipment operability determinations, reportability assessments, and extent-of-condition reviews for selected problems.  The team assessed the backlog of
corrective actions in the maintenance, engineering, and operations departments, to
determine, individually and collectively, if there was an increased risk due to delays in
implementation of corrective actions.  The team further reviewed equipment performance results and assessments documented in completed surveillance procedures, operator log entries, and trend data to determine whether the evaluations
were technically adequate to identify degrading or non-conforming equipment.
The team reviewed the corrective actions associated with selected CRs to determine if
the actions addressed the identified causes of the problems.  The team reviewed CRs for significant repetitive problems to determine if previous corrective actions were
effective.  The team also reviewed Susquehanna
=s timeliness in implementing corrective actions.  The team reviewed the CRs associated with selected non-cited violations (NCVs) and findings to determine if Susquehanna properly evaluated and resolved these
issues.
  2. Assessment
    (a) Identification of Issues
  In general, the team considered the identification of equipment deficiencies at
Susquehanna to be adequate.  There was a low threshold for the identification of
individual issues, 23,000 ARs were written per year, and about 4,000 of those were
sub-classified as CRs.  The housekeeping and cleanliness of the plant was generally good; the general cleanliness of the plant enhanced the ability of personnel to more easily identify equipment deficiencies and monitor equipment for worsening conditions.
 
Notwithstanding, during a tour of the facility, the inspectors observed that high density
concrete shield blocks were stacked on pallets in the vicinity of the Unit 1 recirculation 
  Enclosure
8motor generator sets.  The blocks were pre-staged for work during the upcoming refueling outage, and were in a heavily trafficked area of the turbine building.  There was
a painted warning on the floor, near the pallets, that the floor loading should not exceed 400 pounds per square foot (psf).  When the inspectors asked whether the weight of the blocks was within the rated floor load limit, it was determined that this condition had not
been identified and documented as acceptable.  Initially, Susquehanna personnel
concluded that the blocks exceeded the posted
limit and moved the pallets to reduce the floor loading.  Subsequently, Susquehanna weighed the pallets and blocks and determined that they did not exceed the allowable floor loading.  Based on this evaluation the inspectors concluded the missed identification of this issue was minor. 
The issue was documented in CR 954950.
 
The team also identified that several ARs were not classified as CRs, commensurate
with the safety significance, as required by their procedure (NDAP-QA-0702, "Action Request and Condition Report Process").  The result was that the issues did not go to
the Screening Team, did not receive the necessary management attention, and were not corrected in a timely manner (CR 957319).  In addition, ARs are not normally trended to
allow the identification of an adverse change in performance.  With the exception of the
first example, the below are considered procedure violations of minor significance due to no impact on the related equipment.  As such, these issues are not subject to enforcement action, in accordance with the NRC
=s Enforcement Policy.
Examples include:
AR/CPG/OPS 751412, initiated February 2, 2006, identified that the Low Pressure Injection Permissive setpoint was not changed in the residual heat removal (RHR)
and core spray (CS) operating procedures.  The setpoint was changed in 1999, as
part of a modification; the procedures were not changed until July 2007.  (See Section 4OA2.a.3(d) for additional details.)
AR/OPS/CSHIFT 777335, initiated July 25 2006, identified that an operator started the suppression pool (SP) filter pump contrary to the procedure.  The AR was closed
with no documented corrective actions taken. 
The safety significance is that the operator did not operate the safety-related system
in accordance with the licensee's written procedures and the Technical
Specifications (TS).  The documentation of corrective actions should have included a
determination of the affects of starting of the pump, and counseling of the operator
 
on the requirement to follow procedures.
  AR/CPG 810513, initiated September 16, 2006, identified that the wrong valve numbers were listed for the emergency service water (ESW) system valves for the
"E" EDG.  As of the inspection, the procedure had not been changed. 
The safety significance is that operators may not have been able to use the licensee's written procedure to align the ESW system in support of the operation of
the swing "E" EDG in a timely manner. 
  Enclosure
9  AR/CPG/I&C 938054, initiated December 10, 2007, identified that a functional testing and calibration procedure for the RHR service water radiation monitor could not be performed, as written.  As of the inspection, corrective actions had not been taken.
an inconsistency between the procedures and the design basis for SP cooling was a
CAQ, which resulted in corrective actions not being taken for two years to the time of the
inspection.  Although the inconsistency was identified in 2006, Susquehanna personnel did not recognize that the issue impacted current plant operations; as a result, the issue was not scheduled for resolution in a timely manner.  The team noted that, although
Susquehanna had classified the issue as a CR, it was considered to be "NAQ" - not a
CAQ - and was not scheduled for evaluation until the EPU had been approved.  Refer to
Section 4OA2.a.3(b) for a detailed discussion of the finding.
    (b) Prioritization and Evaluation of Issues
  The team determined that Susquehanna's performance in this area was adequate. 
Notwithstanding the above discussion of some ARs not being classified as CRs, the
station appropriately reviewed those CRs that went to the Screening team and properly classified them for significance.  The discussions about specific topics at the Screening meetings were detailed, and there were no classifications or immediate operability
determinations with which the team disagreed.  The team considered the contributions of
the CARB to add value to the CAP process.  One CARB review was noted to be
particularly insightful with respect to the quality of the causal analysis for CR 773046. 
The CR identified problems with the closing of CRs by the nuclear training department without completing all the required actions.  The team did not identify any items in the operations, engineering, or maintenance backlogs that were risk significant, individually
or collectively.  In addition, the quality of the causal analyses reviewed was generally of
adequate technical detail and scope to identify causal factors and develop effective
corrective actions.  The team noted that the RCA for the NCV from the last PI&R inspection related to scaffolding was effective in that there had not been significant recurrences of inadequate scaffold installations since the evaluation was completed.
 
With regard to operability evaluations, the team observed that, an operability
determination for the PAM level instruments, conducted in response to an inconsistency
between the FSAR and EOPs, determined that the level instruments would be operable.  (The inconsistency between the FSAR and the EOPs is described in detail in section 4OA2.a.3(b).)  During follow-up discussions, the inspectors were told by operations and
engineering personnel that all of the PAM instrumentation together functioned to provide
the needed indications to the operators, and that the RPV level indications were not
needed after the initial entry into the EOPs.  This was not consistent with the requirements for the operability of each individual function of the PAM, as detailed in TS 3.3.3.1.  Although subsequent discussions with the Susquehanna staff determined that
the most (if not all) of the PAM RPV level instruments would indicate post-LOCA, the
initial operability determination and statements during the inspection did not consider
that the PAM level instruments are required to be operable post-accident regardless of whether EOPs have been entered.  This issue was related to the performance 
  Enclosure
10deficiencies discussed in findings 4OA2.a.3(a), (b) and (c), and is not identified as an additional finding.  The issue was entered into the CAP as AR/CR964836.
 
    (c) Effectiveness of Corrective Actions
  No findings of significance were identified in the area of effectiveness of corrective
actions.  The team determined that the effectiveness of corrective actions at
Susquehanna was generally good.  The control of scaffolds was a significant problem during the last PI&R inspection; the team noted that oversight of scaffolds has improved, but station personnel continue to identify examples where the scaffold does not appear
to be built in accordance with the procedure.  In addition, the team identified
weaknesses in the scaffold procedure, such as allowing the installer to approve
deviations from the approved construction.  During the inspection, the procedure was
revised, and plans were developed for engineering to review all current deviations.
  3. Findings
 
  (a) Failure to Adequately Evaluate a Deviation from BWROG EPG/SAG Resulted in an
Inadequate Procedure
  Introduction:  The NRC identified a Green NCV of 10 CFR 50, Appendix B, Criterion V, "Instructions, Procedures, and Drawings," because Susquehanna failed to adequately
 
evaluate a deviation from the Boiling Water Reactor Owner's Group Emergency
Procedure Guidelines / Severe Accident
Guidelines (BWROG EPG/SAG), which resulted in one of the Emergency Operating Procedures (EOPs) being inadequate.
Description:  On January 5, 2006, AR/CR 739371 was initiated to document an inconsistency between the EOPs and assumptions in the Final Safety Analysis Report
(FSAR) regarding the initiation of suppression pool cooling.  Specifically, it was identified
that the assumptions used in evaluating SP temperature response for the most limiting design basis accident (DBA) loss of coolant accident (LOCA) did not appear to be consistent with direction provided in the EOPs.
 
During this inspection, the team noted that the Susquehanna EOPs were not consistent
with the BWROG EPG/SAG.  Specifically, BWROG EPG/SAG, Revision 2, Caution #1, warned the operators that reactor pressure vessel (RPV) level instrumentation may be unreliable if the temperatures near the instrument sensing lines exceeded RPV saturation temperature.  The EPG Bases stated that the purpose of Caution #1 was to
give the operators a chance to evaluate the validity of the RPV level instrumentation, in
order to avoid premature entry into the RPV flooding contingency procedure before it
was appropriate to do so.  Susquehanna did not adequately evaluate the deviation from the generic guidance in the EPG/SAG with respect to the caution.  The Susquehanna EOPs did not use a Caution statement, which would have allowed the operators the
opportunity to evaluate the level instrumentation; but instead, changed the caution to a
procedural step which directed the operators to transition directly to the RPV Flooding
procedure.  Specifically, EO-100-103-1, "Primary Containment Cooling," step DWT-3, 
  Enclosure
11directed the operators to transition to contingency procedure EO-000-114-1, "RPV
Flooding," when drywell temperature exceeded RPV saturation temperature.
The evaluation for the deviation was not completed in accordance with the requirements of procedure NDAP-QA-0330, "Symptom Oriented EOP and EP-DS Program and
Writer's Guide."  The procedure required that all deviations be evaluated to determine if
the deviation was technically justifie
d and appropriate.  Susquehanna documented that the deviation was a minor "difference" from the generic guidelines in 50.59 Safety
Evaluation NL-92-019 (October 29, 1998) and 50.59 Screen 5059-01-976 (July 3, 2002).
The evaluation was based on an overly conservative assumption that all RPV level
instrumentation would be lost after a DBA LOCA.  The reviews did not evaluate the
potential adverse consequences associated with the deviation, including the potential
impact on the SP cooling safety function.  Immediate corrective actions included the
initiation of an informational Night Order to the control room operators explaining the issue, and the cessation of all simulator scenarios that involve the use of EO-100-103-1 until the issue is resolved.
 
The performance deficiency is the failure to adequately evaluate a deviation from the
BWROG EPG/SAG, which resulted in one of the EOPs being inadequate for use by the operators in the event of a DBA LOCA.  Specifically, under some accident conditions, the EOPs would have unnecessarily directed entry into RPV flooding which would have limited the availability of SP cooling and complicated the operators' response to the
 
event.
Analyses:  This performance deficiency is more than minor because it is associated with the Procedure Quality (EOP) attribute of the Mitigating Systems cornerstone and affects the objective to ensure the availability, reliability, and capability of systems that respond
to initiating events to prevent undesirable consequences.  Specifically, the EOP could
have directed entry into the RPV flooding procedure unnecessarily which would have restricted the use of suppression pool cooling and required other actions that would have complicated the operators' response to the event.  The inspectors performed a review of the finding in accordance with NRC Inspection Manual Chapter (IMC) 0609,
"Significance Determination Process (SDP)," Attachment 4, "Phase 1 - Initial Screening
and Characterization of Findings," and determined that the finding screened out as
having very low safety significance (Green), because it was not a design deficiency, did
not result in an actual loss of safety function, and did not screen as potentially risk significant due to external initiating events.
Enforcement:  10 CFR 50, Appendix B, Criterion V, "Instructions, Procedures, and Drawings," states, in part, that activities affecting quality shall be prescribed by
documented procedures appropriate to the circumstances and that the activities shall be accomplished in accordance with the procedures.  Contrary to the above, Emergency Operating Procedure EO-100-103-1, "Primary Containment Cooling," was inadequate, in
that it directed the operators to transition directly to the RPV Flooding procedure when
RPV level instruments may have been available, which resulted in limiting the availability of SP cooling.  However, because the finding was of very low safety significance (Green) 
  Enclosure
12and has been entered into the CAP (AR/CR 962881), this violation is being treated as an NCV, consistent with section VI.A.1 of the NRC Enforcement Policy.
(NCV 05000387/2008006-01; 05000388/2008006-01 - Failure to Adequately Evaluate a Deviation from BWROG EPG/SAG Resulted in an Inadequate EOP)
    (b) Failure to Identify and Correct Inconsistencies Between the FSAR and the EOPs
  Introduction:  The NRC identified a Green NCV of 10 CFR 50, Appendix B, Criterion XVI, "Corrective Action," for the failure to identify that an inconsistency between the
emergency operating procedures and the design basis for SP cooling was a CAQ, which
resulted in corrective actions not being taken for two years to the time of the inspection. 
Although the inconsistency was identified in 2006, Susquehanna personnel did not
recognize that the issue impacted current plant operations; as a result, the issue was not scheduled for resolution in a timely manner.  The assumption in the FSAR for the DBA LOCA stated that SP cooling would be implemented ten minutes after entry into the
EOPs. The EOPs would not have allowed initiation of SP cooling for an extended period
of time. 


Description:  On January 5, 2006, AR/CR 739371 was initiated to document an inconsistency between the EOPs and design basis assumptions for the SP cooling
                                                7
response. The problem was identified during Susquehanna's review in support of the  
    reports, work requests and engineering documents, plant log entries, and results from
extended power uprate (EPU) project. Specifically, Susquehanna Engineering identified
    surveillance tests and maintenance tasks.
that the assumptions used in evaluating SP temperature response for the most limiting
    The team reviewed CRs to assess whether Susquehanna adequately evaluated and
LOCA did not appear to be consistent with direction provided in the EOPs. The team noted that, although Susquehanna personnel had classified the issue as a CR, they did not recognize that the issue impacted current plant operations.  Therefore, it was
    prioritized the identified problems. The CRs reviewed encompassed the full range of
considered to be "NAQ" - not a condition adverse to quality - and was not scheduled for  
    Susquehanna=s causal evaluations, including root cause analyses (RCA - to determine
evaluation until the EPU had been approved.
    the cause and prevent recurrence), apparent cause evaluations (ACE - to obtain a basic
    understanding of the cause), and evaluations (to determine if a problem exists). The
    review included the appropriateness of the assigned significance, the scope and depth
    of the causal analysis, and the timeliness of the resolutions. For significant conditions
    adverse to quality, the team reviewed the effectiveness of the corrective actions to
    prevent recurrence. The team observed meetings of the CR Screening Team - in which
    Susquehanna personnel reviewed new CRs for prioritization, and evaluated preliminary
    corrective action assignments, analyses, and plans. The team also attended meetings
    of the Corrective Action Review Board (CARB) - where senior managers reviewed
    selected evaluations, effectiveness reviews, and extension requests.
    The team reviewed equipment operability determinations, reportability assessments, and
    extent-of-condition reviews for selected problems. The team assessed the backlog of
    corrective actions in the maintenance, engineering, and operations departments, to
    determine, individually and collectively, if there was an increased risk due to delays in
    implementation of corrective actions. The team further reviewed equipment
    performance results and assessments documented in completed surveillance
    procedures, operator log entries, and trend data to determine whether the evaluations
    were technically adequate to identify degrading or non-conforming equipment.
    The team reviewed the corrective actions associated with selected CRs to determine if
    the actions addressed the identified causes of the problems. The team reviewed CRs
    for significant repetitive problems to determine if previous corrective actions were
    effective. The team also reviewed Susquehanna=s timeliness in implementing corrective
    actions. The team reviewed the CRs associated with selected non-cited violations
    (NCVs) and findings to determine if Susquehanna properly evaluated and resolved these
    issues.
2.  Assessment
(a) Identification of Issues
    In general, the team considered the identification of equipment deficiencies at
    Susquehanna to be adequate. There was a low threshold for the identification of
    individual issues, 23,000 ARs were written per year, and about 4,000 of those were
    sub-classified as CRs. The housekeeping and cleanliness of the plant was generally
    good; the general cleanliness of the plant enhanced the ability of personnel to more
    easily identify equipment deficiencies and monitor equipment for worsening conditions.
    Notwithstanding, during a tour of the facility, the inspectors observed that high density
    concrete shield blocks were stacked on pallets in the vicinity of the Unit 1 recirculation
                                                                                          Enclosure


The Susquehanna FSAR, Section 6.2.1.1.3, stated that the maximum SP temperature would result from a reactor recirculation suction line break. The drywell pressure and  
                                            8
temperature response analyses assumed that RHR heat exchangers were activated
motor generator sets. The blocks were pre-staged for work during the upcoming
about ten minutes after entry into the EOPs to remove energy from the drywell by
refueling outage, and were in a heavily trafficked area of the turbine building. There was
cooling the SP. The CR identified that, in the event of a DBA LOCA, the EOPs would
a painted warning on the floor, near the pallets, that the floor loading should not exceed
direct operators to implement the RPV flooding procedure (EO-000-114) to maintain
400 pounds per square foot (psf). When the inspectors asked whether the weight of the
adequate core cooling, and this required that
blocks was within the rated floor load limit, it was determined that this condition had not
all available RHR flow be used to flood the RPV up to the steam lines. The initiator's concern was that this would delay establishing
been identified and documented as acceptable. Initially, Susquehanna personnel
flow through a RHR heat exchanger for SP cooling, because of the unique design of the RHR system at Susquehanna, and therefore w
concluded that the blocks exceeded the posted limit and moved the pallets to reduce the
ould be inconsistent with the accident analyses assumptions. In addition, the CR stated that it was assumed in the EOPs that all RPV water level indications would be unreliable and therefore unavailable for this scenario. Susquehanna personnel informed the team that they had not evaluated the  
floor loading. Subsequently, Susquehanna weighed the pallets and blocks and
issues documented in the CR, at the time it was initiated, because they had assumed
determined that they did not exceed the allowable floor loading. Based on this
that they were only associated with EPU and not current plant operation. Immediate
evaluation the inspectors concluded the missed identification of this issue was minor.
corrective actions included the start of an evaluation during the inspection of the identified inconsistency for SP cooling, and additional guidance to the operators.
The issue was documented in CR 954950.
  Enclosure
The team also identified that several ARs were not classified as CRs, commensurate
13 The performance deficiency is the failure to properly categorize the inconsistency
with the safety significance, as required by their procedure (NDAP-QA-0702, Action
between the FSAR and the EOPs as a CAQ, which resulted in the deficiency not being corrected in a timely manner commensurate with its safety significance. 
Request and Condition Report Process). The result was that the issues did not go to
the Screening Team, did not receive the necessary management attention, and were not
Analyses:  The performance deficiency is more than minor because it is associated with the Design Control attribute of the Mitigating Systems cornerstone and affects the  
corrected in a timely manner (CR 957319). In addition, ARs are not normally trended to
objective to ensure the availability, reliability, and capability of systems that respond to initiating events to prevent undesirable consequences. Specifically, in the event of a DBA LOCA, SP cooling would not be initiated within the time frame assumed in the  
allow the identification of an adverse change in performance. With the exception of the
FSAR, which could affect the capability of the system to perform its safety function
first example, the below are considered procedure violations of minor significance due to
consistent with the design basis. The inspectors performed a review of the finding in
no impact on the related equipment. As such, these issues are not subject to
accordance with IMC 0609, and determined that the finding screened out as having very
enforcement action, in accordance with the NRC=s Enforcement Policy.
low safety significance (Green) because it was not a design deficiency, did not result in an actual loss of safety function, and did not screen as potentially risk significant due to
Examples include:
external initiating events.  
C    AR/CPG/OPS 751412, initiated February 2, 2006, identified that the Low Pressure
    Injection Permissive setpoint was not changed in the residual heat removal (RHR)
    and core spray (CS) operating procedures. The setpoint was changed in 1999, as
    part of a modification; the procedures were not changed until July 2007. (See
    Section 4OA2.a.3(d) for additional details.)
C    AR/OPS/CSHIFT 777335, initiated July 25 2006, identified that an operator started
    the suppression pool (SP) filter pump contrary to the procedure. The AR was closed
    with no documented corrective actions taken.
    The safety significance is that the operator did not operate the safety-related system
    in accordance with the licensees written procedures and the Technical
    Specifications (TS). The documentation of corrective actions should have included a
    determination of the affects of starting of the pump, and counseling of the operator
    on the requirement to follow procedures.
C    AR/CPG 810513, initiated September 16, 2006, identified that the wrong valve
    numbers were listed for the emergency service water (ESW) system valves for the
    E EDG. As of the inspection, the procedure had not been changed.
    The safety significance is that operators may not have been able to use the
    licensees written procedure to align the ESW system in support of the operation of
    the swing E EDG in a timely manner.
                                                                                    Enclosure


                                                9
This performance deficiency has a cross-cutting aspect in the area of Problem
    C    AR/CPG/I&C 938054, initiated December 10, 2007, identified that a functional testing
Identification and Resolution (PI&R), Corrective Action Program (CAP), because Susquehanna did not identify that the inconsistency documented in the CR should have been categorized as a CAQ, commensurate with its safety significance. [P.1(a)]
        and calibration procedure for the RHR service water radiation monitor could not be
Enforcement:  10 CFR 50, Appendix B, Criterion XVI, "Corrective Action," states, in part, that conditions adverse to quality shall be promptly identified and corrected. Contrary to  
        performed, as written. As of the inspection, corrective actions had not been taken.
the above, Susquehanna failed to identify that the nonconformance identified in AR/CR 739371, January 2006, was a CAQ; this resulted in the condition not being corrected for over two years.  However, because the finding was of very low safety significance
    an inconsistency between the procedures and the design basis for SP cooling was a
(Green) and has been entered into the corrective action program (AR/CR 959670), this
    CAQ, which resulted in corrective actions not being taken for two years to the time of the
violation is being treated as an NCV, consistent with section VI.A.1 of the NRC
    inspection. Although the inconsistency was identified in 2006, Susquehanna personnel
    did not recognize that the issue impacted current plant operations; as a result, the issue
    was not scheduled for resolution in a timely manner. The team noted that, although
    Susquehanna had classified the issue as a CR, it was considered to be NAQ - not a
    CAQ - and was not scheduled for evaluation until the EPU had been approved. Refer to
    Section 4OA2.a.3(b) for a detailed discussion of the finding.
(b) Prioritization and Evaluation of Issues
    The team determined that Susquehannas performance in this area was adequate.
    Notwithstanding the above discussion of some ARs not being classified as CRs, the
    station appropriately reviewed those CRs that went to the Screening team and properly
    classified them for significance. The discussions about specific topics at the Screening
    meetings were detailed, and there were no classifications or immediate operability
    determinations with which the team disagreed. The team considered the contributions of
    the CARB to add value to the CAP process. One CARB review was noted to be
    particularly insightful with respect to the quality of the causal analysis for CR 773046.
    The CR identified problems with the closing of CRs by the nuclear training department
    without completing all the required actions. The team did not identify any items in the
    operations, engineering, or maintenance backlogs that were risk significant, individually
    or collectively. In addition, the quality of the causal analyses reviewed was generally of
    adequate technical detail and scope to identify causal factors and develop effective
    corrective actions. The team noted that the RCA for the NCV from the last PI&R
    inspection related to scaffolding was effective in that there had not been significant
    recurrences of inadequate scaffold installations since the evaluation was completed.
    With regard to operability evaluations, the team observed that, an operability
    determination for the PAM level instruments, conducted in response to an inconsistency
    between the FSAR and EOPs, determined that the level instruments would be operable.
    (The inconsistency between the FSAR and the EOPs is described in detail in section
    4OA2.a.3(b).) During follow-up discussions, the inspectors were told by operations and
    engineering personnel that all of the PAM instrumentation together functioned to provide
    the needed indications to the operators, and that the RPV level indications were not
    needed after the initial entry into the EOPs. This was not consistent with the
    requirements for the operability of each individual function of the PAM, as detailed in TS
    3.3.3.1. Although subsequent discussions with the Susquehanna staff determined that
    the most (if not all) of the PAM RPV level instruments would indicate post-LOCA, the
    initial operability determination and statements during the inspection did not consider
    that the PAM level instruments are required to be operable post-accident regardless of
    whether EOPs have been entered. This issue was related to the performance
                                                                                        Enclosure


Enforcement Policy.   
                                              10
(NCV 05000387/2008006-02; 05000388/2008006-02 - Failure to Identify and Correct
    deficiencies discussed in findings 4OA2.a.3(a), (b) and (c), and is not identified as an
Inconsistencies Between the FSAR and the EOPs)  
    additional finding. The issue was entered into the CAP as AR/CR964836.
  (c) Effectiveness of Corrective Actions
    No findings of significance were identified in the area of effectiveness of corrective
    actions. The team determined that the effectiveness of corrective actions at
    Susquehanna was generally good. The control of scaffolds was a significant problem
    during the last PI&R inspection; the team noted that oversight of scaffolds has improved,
    but station personnel continue to identify examples where the scaffold does not appear
    to be built in accordance with the procedure. In addition, the team identified
    weaknesses in the scaffold procedure, such as allowing the installer to approve
    deviations from the approved construction. During the inspection, the procedure was
    revised, and plans were developed for engineering to review all current deviations.
3.  Findings
(a) Failure to Adequately Evaluate a Deviation from BWROG EPG/SAG Resulted in an
    Inadequate Procedure
    Introduction: The NRC identified a Green NCV of 10 CFR 50, Appendix B, Criterion V,
    Instructions, Procedures, and Drawings, because Susquehanna failed to adequately
    evaluate a deviation from the Boiling Water Reactor Owners Group Emergency
    Procedure Guidelines / Severe Accident Guidelines (BWROG EPG/SAG), which
    resulted in one of the Emergency Operating Procedures (EOPs) being inadequate.
    Description: On January 5, 2006, AR/CR 739371 was initiated to document an
    inconsistency between the EOPs and assumptions in the Final Safety Analysis Report
    (FSAR) regarding the initiation of suppression pool cooling. Specifically, it was identified
    that the assumptions used in evaluating SP temperature response for the most limiting
    design basis accident (DBA) loss of coolant accident (LOCA) did not appear to be
    consistent with direction provided in the EOPs.
    During this inspection, the team noted that the Susquehanna EOPs were not consistent
    with the BWROG EPG/SAG. Specifically, BWROG EPG/SAG, Revision 2, Caution #1,
    warned the operators that reactor pressure vessel (RPV) level instrumentation may be
    unreliable if the temperatures near the instrument sensing lines exceeded RPV
    saturation temperature. The EPG Bases stated that the purpose of Caution #1 was to
    give the operators a chance to evaluate the validity of the RPV level instrumentation, in
    order to avoid premature entry into the RPV flooding contingency procedure before it
    was appropriate to do so. Susquehanna did not adequately evaluate the deviation from
    the generic guidance in the EPG/SAG with respect to the caution. The Susquehanna
    EOPs did not use a Caution statement, which would have allowed the operators the
    opportunity to evaluate the level instrumentation; but instead, changed the caution to a
    procedural step which directed the operators to transition directly to the RPV Flooding
    procedure. Specifically, EO-100-103-1, Primary Containment Cooling, step DWT-3,
                                                                                          Enclosure


    (c) Failure to Accurately Model the Simulator for RPV Water Level Instrumentation
                                          11
  Introduction:  The NRC identified a Green NCV of 10 CFR 55.46(c)(1), "Plant Referenced Simulators," because the Susquehanna plant-referenced simulator did not
directed the operators to transition to contingency procedure EO-000-114-1, RPV
accurately model RPV level instrument response following a DBA LOCA. Specifically, the RPV level instruments in the simulator were programmed to fail high after a LOCA,  
Flooding, when drywell temperature exceeded RPV saturation temperature.
and the expected plant response is that the instruments should indicate properly.  
The evaluation for the deviation was not completed in accordance with the requirements
Description:  As part of the team's follow-up on the issues in AR/CR 739371, the inspectors questioned the concern stated in the CR, that the operators would need to
of procedure NDAP-QA-0330, Symptom Oriented EOP and EP-DS Program and
enter the RPV flooding procedure during a DBA LOCA due to a loss of valid RPV level
Writers Guide. The procedure required that all deviations be evaluated to determine if
instrumentation.  The inspectors reviewed the Susquehanna specific EOPs and supporting documents, and determined that the Susquehanna EOP Plant Specific 
the deviation was technically justified and appropriate. Susquehanna documented that
  Enclosure
the deviation was a minor difference from the generic guidelines in 50.59 Safety
14Technical Guideline (PSTG) description of the expected response of the RPV level instrument response to LOCA events, was based on analysis, EC-SIMU-1001,  
Evaluation NL-92-019 (October 29, 1998) and 50.59 Screen 5059-01-976 (July 3, 2002).
"Evaluation of Simulator Level Instrument Response to Large LOCA," dated May 4, 1994.  The analysis was performed to determine if the observed simulator response during a large break LOCA (RPV level instrumentation off-scale high) was consistent
The evaluation was based on an overly conservative assumption that all RPV level
with the expected plant response. The analysis assumed that the drywell would
instrumentation would be lost after a DBA LOCA. The reviews did not evaluate the
experience superheated conditions, which would cause RPV water level instrumentation
potential adverse consequences associated with the deviation, including the potential
reference leg flashing and a subsequent loss of all RPV level indication.  The analysis concluded that the simulator response reasonably predicted the expected actual plant response during a large break LOCA event.  The expected plant response, as stated in
impact on the SP cooling safety function. Immediate corrective actions included the
the analysis, was incorrect; in that a LOCA would not always cause a loss of all RPV
initiation of an informational Night Order to the control room operators explaining the
level instruments.  
issue, and the cessation of all simulator scenarios that involve the use of EO-100-103-1
On January 29, 2008, the inspectors observed two scenarios in the simulator to evaluate the response to a DBA LOCA, with all safe
until the issue is resolved.
ty systems available.  The inspectors observed that the RPV level instruments did indicate off-scale high shortly after the
The performance deficiency is the failure to adequately evaluate a deviation from the
initiation of the event, consistent with the analysis. The inspectors questioned the basis
BWROG EPG/SAG, which resulted in one of the EOPs being inadequate for use by the
of the analysis; specifically, why Susquehanna believed that the level instruments would
operators in the event of a DBA LOCA. Specifically, under some accident conditions,
not be available after a DBA LOCA event.  Subsequently, Susquehanna determined that the RPV level instrument reference legs were not expected to routinely flash during a DBA LOCA, and that the analysis had been based on an overly conservative assumption
the EOPs would have unnecessarily directed entry into RPV flooding which would have
that the drywell would always reach superheated conditions post-LOCA. Immediate
limited the availability of SP cooling and complicated the operators response to the
corrective actions included the initiation of an informational Night Order to the control
event.
room operators explaining the issue, and the cessation of all simulator scenarios that
Analyses: This performance deficiency is more than minor because it is associated with
the Procedure Quality (EOP) attribute of the Mitigating Systems cornerstone and affects
the objective to ensure the availability, reliability, and capability of systems that respond
to initiating events to prevent undesirable consequences. Specifically, the EOP could
have directed entry into the RPV flooding procedure unnecessarily which would have
restricted the use of suppression pool cooling and required other actions that would have
complicated the operators response to the event. The inspectors performed a review of
the finding in accordance with NRC Inspection Manual Chapter (IMC) 0609,
Significance Determination Process (SDP), Attachment 4, Phase 1 - Initial Screening
and Characterization of Findings, and determined that the finding screened out as
having very low safety significance (Green), because it was not a design deficiency, did
not result in an actual loss of safety function, and did not screen as potentially risk
significant due to external initiating events.
Enforcement: 10 CFR 50, Appendix B, Criterion V, Instructions, Procedures, and
Drawings, states, in part, that activities affecting quality shall be prescribed by
documented procedures appropriate to the circumstances and that the activities shall be
accomplished in accordance with the procedures. Contrary to the above, Emergency
Operating Procedure EO-100-103-1, Primary Containment Cooling, was inadequate, in
that it directed the operators to transition directly to the RPV Flooding procedure when
RPV level instruments may have been available, which resulted in limiting the availability
of SP cooling. However, because the finding was of very low safety significance (Green)
                                                                                        Enclosure


involve the use of EO-100-103-1 until the issue is resolved.  
                                              12
The performance deficiency is that Susquehanna did not ensure that the plant  
    and has been entered into the CAP (AR/CR 962881), this violation is being treated as an
referenced simulator accurately modeled the expected plant response for RPV level  
    NCV, consistent with section VI.A.1 of the NRC Enforcement Policy.
    (NCV 05000387/2008006-01; 05000388/2008006-01 - Failure to Adequately Evaluate
    a Deviation from BWROG EPG/SAG Resulted in an Inadequate EOP)
(b) Failure to Identify and Correct Inconsistencies Between the FSAR and the EOPs
    Introduction: The NRC identified a Green NCV of 10 CFR 50, Appendix B, Criterion XVI,
    Corrective Action, for the failure to identify that an inconsistency between the
    emergency operating procedures and the design basis for SP cooling was a CAQ, which
    resulted in corrective actions not being taken for two years to the time of the inspection.
    Although the inconsistency was identified in 2006, Susquehanna personnel did not
    recognize that the issue impacted current plant operations; as a result, the issue was not
    scheduled for resolution in a timely manner. The assumption in the FSAR for the DBA
    LOCA stated that SP cooling would be implemented ten minutes after entry into the
    EOPs. The EOPs would not have allowed initiation of SP cooling for an extended period
    of time.
    Description: On January 5, 2006, AR/CR 739371 was initiated to document an
    inconsistency between the EOPs and design basis assumptions for the SP cooling
    response. The problem was identified during Susquehannas review in support of the
    extended power uprate (EPU) project. Specifically, Susquehanna Engineering identified
    that the assumptions used in evaluating SP temperature response for the most limiting
    LOCA did not appear to be consistent with direction provided in the EOPs. The team
    noted that, although Susquehanna personnel had classified the issue as a CR, they did
    not recognize that the issue impacted current plant operations. Therefore, it was
    considered to be NAQ - not a condition adverse to quality - and was not scheduled for
    evaluation until the EPU had been approved.
    The Susquehanna FSAR, Section 6.2.1.1.3, stated that the maximum SP temperature
    would result from a reactor recirculation suction line break. The drywell pressure and
    temperature response analyses assumed that RHR heat exchangers were activated
    about ten minutes after entry into the EOPs to remove energy from the drywell by
    cooling the SP. The CR identified that, in the event of a DBA LOCA, the EOPs would
    direct operators to implement the RPV flooding procedure (EO-000-114) to maintain
    adequate core cooling, and this required that all available RHR flow be used to flood the
    RPV up to the steam lines. The initiators concern was that this would delay establishing
    flow through a RHR heat exchanger for SP cooling, because of the unique design of the
    RHR system at Susquehanna, and therefore would be inconsistent with the accident
    analyses assumptions. In addition, the CR stated that it was assumed in the EOPs that
    all RPV water level indications would be unreliable and therefore unavailable for this
    scenario. Susquehanna personnel informed the team that they had not evaluated the
    issues documented in the CR, at the time it was initiated, because they had assumed
    that they were only associated with EPU and not current plant operation. Immediate
    corrective actions included the start of an evaluation during the inspection of the
    identified inconsistency for SP cooling, and additional guidance to the operators.
                                                                                        Enclosure


instrumentation after a DBA LOCA, resulting in negative training of the licensed
                                              13
operators.
    The performance deficiency is the failure to properly categorize the inconsistency
Analyses:  This performance deficiency is more than minor because it is associated with the Human Performance attribute of the Mitigating Systems cornerstone and affects the objective to ensure the availability, reliability, and capability of systems that respond to
    between the FSAR and the EOPs as a CAQ, which resulted in the deficiency not being
initiating events to prevent undesirable consequences.  Specifically, the incorrect
     corrected in a timely manner commensurate with its safety significance.
modeling of the Susquehanna plant referenced simulator introduces negative operator training that could affect the ability of the operators (a mitigating system) to take the appropriate actions during an actual even
    Analyses: The performance deficiency is more than minor because it is associated with
t.  The simulator training conditioned the operators to expect the level instruments to be unavailable during events that cause
    the Design Control attribute of the Mitigating Systems cornerstone and affects the
drywell temperatures to reach or exceed RPV saturation temperature.  As a result,
    objective to ensure the availability, reliability, and capability of systems that respond to
during an actual event, the operators could prematurely transition into the RPV flooding procedure when the RPV level instruments should be providing valid indication.  The inspectors evaluated the finding in accordance with IMC 0609, Appendix I, "Licensed
    initiating events to prevent undesirable consequences. Specifically, in the event of a
Operator Requalification Significance Determination Process."  The finding was
    DBA LOCA, SP cooling would not be initiated within the time frame assumed in the
determined to be of very low safety significance (Green) because it is not related to
    FSAR, which could affect the capability of the system to perform its safety function
operator performance during requalification, it is related to simulator fidelity, and could
    consistent with the design basis. The inspectors performed a review of the finding in
have a negative impact on operator actions. 
    accordance with IMC 0609, and determined that the finding screened out as having very
  Enclosure
    low safety significance (Green) because it was not a design deficiency, did not result in
15 Enforcement:  10 CFR 55.46(c)(1), "Plant Referenced Simulators," states, in part, that a plant referenced simulator must demonstrate expected plant response to normal, transient, and accident conditions.  Contrary to the above, as of January 2008, the Susquehanna plant referenced simulator did not accurately demonstrate the actual
    an actual loss of safety function, and did not screen as potentially risk significant due to
expected plant response of the RPV water level instrumentation following a DBA LOCA,  
    external initiating events.
which could result in negative operator training.  However, because the finding was of
    This performance deficiency has a cross-cutting aspect in the area of Problem
very low safety significance (Green) and has been entered into the CAP (AR/CR 962881), this violation is being treated as an NCV, consistent with section VI.A.1 of the NRC Enforcement Policy.  (NCV 05000387/2008006-03; 05000388/2008006-03 - Failure to Accurately Model
    Identification and Resolution (PI&R), Corrective Action Program (CAP), because
 
    Susquehanna did not identify that the inconsistency documented in the CR should have
the Simulator for RPV Water Level Instrumentation)
    been categorized as a CAQ, commensurate with its safety significance. [P.1(a)]
     (d) Failure to Identify and Correct a Setpoint Error in the RHR and CS Operating
    Enforcement: 10 CFR 50, Appendix B, Criterion XVI, Corrective Action, states, in part,
Procedures
    that conditions adverse to quality shall be promptly identified and corrected. Contrary to
 
    the above, Susquehanna failed to identify that the nonconformance identified in AR/CR
Introduction:  The NRC identified a Green NCV of 10 CFR 50, Appendix B, Criterion XVI, "Corrective Action," for the failure to identify that a setpoint error in the operating procedures for safety-related systems was a CAQ, resulting in the procedures not being corrected in a timely manner.  Specifically, in February 2006, Susquehanna personnel
    739371, January 2006, was a CAQ; this resulted in the condition not being corrected for
identified an incorrect setpoint for the low pressure injection permissive interlock in the
    over two years. However, because the finding was of very low safety significance
 
    (Green) and has been entered into the corrective action program (AR/CR 959670), this
RHR and CS systems operating procedures and associated "hard cards"; however, the procedures were not revised until July 2007 due to the issue being screened as low
    violation is being treated as an NCV, consistent with section VI.A.1 of the NRC
 
    Enforcement Policy.
priority and not a condition adverse to quality (CAQ).
    (NCV 05000387/2008006-02; 05000388/2008006-02 - Failure to Identify and Correct
Description:  On February 11, 2006, an AR was written to identify that the low pressure injection permissive setpoint in the RHR and CS operating procedures, and the
    Inconsistencies Between the FSAR and the EOPs)
associated operator "hard cards," was incorrect.  The correct setpoint is 420 pounds per
(c) Failure to Accurately Model the Simulator for RPV Water Level Instrumentation
square inch gage (psig), but the procedures still had the previous setpoint of 436 psig.  The setpoint had been changed in 1999 as part of a modification.  The procedures were not revised until July 16, 2007, 17 months after the deficiency was identified in an AR.  In
    Introduction: The NRC identified a Green NCV of 10 CFR 55.46(c)(1), Plant
addition, the inspectors noted that the setpoint in the procedures (436 psig) was not
    Referenced Simulators, because the Susquehanna plant-referenced simulator did not
within the allowable tolerance (407-433 psig) listed in the Susquehanna TS, Section
    accurately model RPV level instrument response following a DBA LOCA. Specifically,
 
    the RPV level instruments in the simulator were programmed to fail high after a LOCA,
3.3.5.1, "Emergency Core Cooling System (ECCS) Instrumentation."
    and the expected plant response is that the instruments should indicate properly.
 
    Description: As part of the teams follow-up on the issues in AR/CR 739371, the
When the AR was initiated, it was sub-classified as AR/CPG/OPS; that is, assigned to the Central Procedures Group and identified as an Operations procedure.  It was not
    inspectors questioned the concern stated in the CR, that the operators would need to
recognized that deficient operating procedures for safety-related systems may be a CAQ
    enter the RPV flooding procedure during a DBA LOCA due to a loss of valid RPV level
and that the AR should have been classified as a Condition Report.  The affected
    instrumentation. The inspectors reviewed the Susquehanna specific EOPs and
section in the procedures was the verification of the response of the systems to an
    supporting documents, and determined that the Susquehanna EOP Plant Specific
automatic initiation signal.  For example, the Unit 1 RHR procedure OP-149-001, "RHR System," Section 2.2, noted that "No operator action is required unless an automatic action failed to occur ...  At 436 psig decreasing Reactor pressure, RHR INJ OB ISO [injection outboard isolation] HV-151-F015A & B OPEN."  If the valves did not open at
                                                                                          Enclosure
the specified pressure in the procedure and "hard card," the operator may have diverted their attention unnecessarily and attempted to open the valve manually, even though the 
  Enclosure
16interlock would not have been satisfied (420 psig) and the valve would not open in accordance with the plant design. 
 
The pressure switches were changed in 1999, as part of a Unit 1 plant modification (Design Change Package (DCP) 97-9075); Unit 2 switches were changed by DCP
97-9076.  The modification replaced the existing pressure switches with Barton pressure
indicating switches, because of improved accuracy.  The low pressure injection
permissive interlock prevents the CS and RHR injection valves from opening until
reactor pressure has decreased to the RHR and CS systems design pressure, to prevent over pressurization of the RHR and CS systems.  The DCP identified the specific RHR and CS operating procedures as needing to be changed.  Immediate
corrective actions included the initiation of a new CR to evaluate the other pending
procedure changes to determine if their priority should be revised.
 
The performance deficiency involved a failure to identify and correct a CAQ, the incorrect setpoint, in a timely manner commensurate with its safety significance. The
inspectors concluded this action was untimely because the modification process would have revised these procedures prior to the modification being accepted by operations
personnel. 
Analysis: The performance deficiency is more than minor because it is associated with the Procedure Quality attribute of the Mitigating Systems cornerstone and affects the  
objective to ensure the availability, reliability, and capability of systems that respond to  
initiating events to prevent undesirable consequences.   Specifically, the incorrect
setpoint reference in the procedure impacted the reliability of operator response to the event in that it could delay operator actions or result in misoperation of equipment. The inspectors performed a review of the finding in accordance with NRC Inspection Manual
Chapter (IMC) 0609, "Significance Determination Process (SDP)," Attachment 4, "Phase
1 - Initial Screening and Characterization of Findings."  The inspectors determined that  
the finding screened out as having very low safety significance (Green), because it was not a design deficiency, did not result in an actual loss of safety function, and did not screen as potentially risk significant due to external initiating events  
 
This performance deficiency has a Cross-Cutting aspect in the area of PI&R, CAP,  
because Susquehanna did not identify that a setpoint error in operating procedures for
safety-related systems was a CAQ, commensurate with its safety significance. [P.1(a)]  
Enforcement: 10 CFR 50, Appendix B, Criterion XVI, "Corrective Action," states, in part, that conditions adverse to quality shall be promptly identified and corrected. Contrary to  
the above, from 1999, when the pressure switches were replaced and the setpoint was
changed, until 2006, when AR 751412 was written, Susquehanna had failed to identify that the setpoint was wrong for the low pressure injection permissive interlock in the operating procedures for RHR and CS.  Subsequently, on February 11, 2006, when
Susquehanna personnel initiated and approved AR 751412, they failed to identify that
the stated deficiency was a CAQ, which resulted in untimely corrective actions. 
Susquehanna considered this to be a procedure change and not a CAQ, and classified the AR as a CPG versus a CR.  As such, the procedures were not changed until July 16, 
  Enclosure
172007, 17 months after the condition was identified and eight years after the setpoint was changed in the plant.  Because this finding is of very low safety significance (Green), and  
was entered into the Susquehanna CAP (AR/CR 956917) this violation is being treated as a Non-Cited Violation (NCV) consistent with Section VI.A.1 of the NRC Enforcement  
Policy. (NCV 05000387/2008006-04; 05000388/2008006-04 - Failure to Identify and Correct  
a Setpoint Error in the RHR and CS Operating Procedures)  
  b. Assessment of the Use of Operating Experience
 
  1. Inspection Scope
  The team reviewed a sample of operating experience (OE) issues for applicability to Susquehanna, and for the associated actions.  The documents were reviewed to ensure that underlying problems associated with the issues were appropriately considered for  
resolution.  The team also reviewed how Susquehanna considered OE for applicability in causal evaluations.
 
Prior to the start of the inspection, the inspectors noted a potential negative trend in the
number of issues associated with reactivity management. In accordance with the Inspection Procedure, the inspectors increased the scope of the review to determine if
there was an adverse trend in the area of reactivity management over the past five years.  The inspectors reviewed select ARs and CRs associated with the control rod
 
drive system, control rod problems, human performance issues, and the spent fuel pool; the inspectors review included how Susquehanna had incorporated applicable OE for
these specific systems and human performance issues into the CAP.  The inspectors interviewed selected licensee staff.  
  2. Assessment
  In general, OE was effectively used at the station.  The inspectors noted that OE was
reviewed during the causal evaluation process and incorporated, as appropriate, into the
development of the associated corrective actions.  The inspectors noted that OE was
frequently used in work packages and pre-job briefs.  The team did not identify any
significant deficiencies within the sample reviewed.  The team did not identify a negative trend nor any significant problems with the control of activities associated with reactivity management.  
 
  3. Findings
  No findings of significance were identified in the area of operating experience.
  c. Assessment of Self-Assessments and Audits
 
  1. Inspection Scope
 
  Enclosure
18The team reviewed a sample of departmental self-assessments, CAP trend reports, and Quality Assurance (QA) audits, including QA's most recent audit of the CAP.  The team
also reviewed the latest internal assessment of the safety culture at Susquehanna, conducted in October 2006.  The reviews were performed to determine if problems identified through these evaluations were entered into the CAP system, and whether the  
corrective actions were properly completed to resolve the deficiencies.  The
effectiveness of the audits and self-assessments was evaluated by comparing audit and
self-assessment results
against self-revealing and NRC-identified findings, and observations during the inspection.
  2. Assessment
  The team considered the quality of the audits and self-assessments to be thorough and  
critical.  ARs were initiated for issues identified by QA and the self-assessments.  The
Susquehanna 2006 "Comprehensive Cultural Assessment" Report consisted of a safety culture survey and interviews.  The cultural assessment report identified some
weaknesses at the station, which were entered into the CAP.  The team did not identify
any results that were inconsistent with Susquehanna's conclusions.


  3. Findings
                                            14
  No findings of significance were identified in the area of audits and self-assessments.  
Technical Guideline (PSTG) description of the expected response of the RPV level
instrument response to LOCA events, was based on analysis, EC-SIMU-1001,
d. Assessment of Safety Conscious Work Environment
Evaluation of Simulator Level Instrument Response to Large LOCA, dated May 4,
    1. Inspection Scope
1994. The analysis was performed to determine if the observed simulator response
  To evaluate the safety conscious work environment (SCWE) at Susquehanna, during interviews and discussions with station personnel, the team assessed the workers
during a large break LOCA (RPV level instrumentation off-scale high) was consistent
willingness to enter issues into the CAP and to raise safety issues to their management and/or to the NRC. The inspectors also
with the expected plant response. The analysis assumed that the drywell would
interviewed the Employee Concerns Program (ECP) representative to determine if employees were aware of the program and had
experience superheated conditions, which would cause RPV water level instrumentation
used it to raise concerns. The team reviewed a sample of the ECP files to ensure that  
reference leg flashing and a subsequent loss of all RPV level indication. The analysis
issues were entered into the corrective action program, as appropriate.  
concluded that the simulator response reasonably predicted the expected actual plant
response during a large break LOCA event. The expected plant response, as stated in
  2. Assessment
the analysis, was incorrect; in that a LOCA would not always cause a loss of all RPV
  Based on interviews, observations of plant activities, and reviews of the ARs and ECP,
level instruments.
the inspectors determined that the site personnel were willing to raise safety issues and
On January 29, 2008, the inspectors observed two scenarios in the simulator to evaluate
document them in ARs. Individuals actively
the response to a DBA LOCA, with all safety systems available. The inspectors
utilized the AR system, as evidenced by the number and significance of issues entered into the program. The inspectors noted that ARs were written by a variety of personnel, from workers to managers.  ECP evaluations were thorough and appropriate actions were taken to address issues.  
observed that the RPV level instruments did indicate off-scale high shortly after the
initiation of the event, consistent with the analysis. The inspectors questioned the basis
of the analysis; specifically, why Susquehanna believed that the level instruments would
not be available after a DBA LOCA event. Subsequently, Susquehanna determined that
the RPV level instrument reference legs were not expected to routinely flash during a
DBA LOCA, and that the analysis had been based on an overly conservative assumption
that the drywell would always reach superheated conditions post-LOCA. Immediate
corrective actions included the initiation of an informational Night Order to the control
room operators explaining the issue, and the cessation of all simulator scenarios that
involve the use of EO-100-103-1 until the issue is resolved.
The performance deficiency is that Susquehanna did not ensure that the plant
referenced simulator accurately modeled the expected plant response for RPV level
instrumentation after a DBA LOCA, resulting in negative training of the licensed
operators.
Analyses: This performance deficiency is more than minor because it is associated with
the Human Performance attribute of the Mitigating Systems cornerstone and affects the
objective to ensure the availability, reliability, and capability of systems that respond to
initiating events to prevent undesirable consequences. Specifically, the incorrect
modeling of the Susquehanna plant referenced simulator introduces negative operator
training that could affect the ability of the operators (a mitigating system) to take the
appropriate actions during an actual event. The simulator training conditioned the
operators to expect the level instruments to be unavailable during events that cause
drywell temperatures to reach or exceed RPV saturation temperature. As a result,
during an actual event, the operators could prematurely transition into the RPV flooding
procedure when the RPV level instruments should be providing valid indication. The
inspectors evaluated the finding in accordance with IMC 0609, Appendix I, Licensed
Operator Requalification Significance Determination Process. The finding was
determined to be of very low safety significance (Green) because it is not related to
operator performance during requalification, it is related to simulator fidelity, and could
have a negative impact on operator actions.
                                                                                      Enclosure


  3. Findings
                                              15
  No findings of significance were identified related to the SCWE at Susquehanna
    Enforcement: 10 CFR 55.46(c)(1), Plant Referenced Simulators, states, in part, that a
  Enclosure
    plant referenced simulator must demonstrate expected plant response to normal,
19 4OA6 Meetings, Including Exit
    transient, and accident conditions. Contrary to the above, as of January 2008, the
:  On February 1, 2008, the team presented the inspection results to Mr. B. McKinney, Senior Vice President, and to other members of the Susquehanna staff, who
    Susquehanna plant referenced simulator did not accurately demonstrate the actual
acknowledged the findings. The team confirmed that no proprietary information
    expected plant response of the RPV water level instrumentation following a DBA LOCA,
reviewed during the inspection was retained.  
    which could result in negative operator training. However, because the finding was of
ATTACHMENT:
    very low safety significance (Green) and has been entered into the CAP (AR/CR
  Supplemental Information
    962881), this violation is being treated as an NCV, consistent with section VI.A.1 of the
In addition to the documentation that the team reviewed (listed in the Attachment),
    NRC Enforcement Policy.
copies of information requests given to the licensee are in ADAMS, under accession
    (NCV 05000387/2008006-03; 05000388/2008006-03 - Failure to Accurately Model
number ML080430585.
    the Simulator for RPV Water Level Instrumentation)
  Attachment
(d) Failure to Identify and Correct a Setpoint Error in the RHR and CS Operating
A-1ATTACHMENT - SUPPLEMENTAL INFORMATION
    Procedures
  KEY POINTS OF CONTACT
    Introduction: The NRC identified a Green NCV of 10 CFR 50, Appendix B, Criterion XVI,
  Licensee Personnel
    Corrective Action, for the failure to identify that a setpoint error in the operating
:  M. Adelizzi, Risk Engineer
    procedures for safety-related systems was a CAQ, resulting in the procedures not being
N. D'Angelo, Manager, Station Engineering C. Gannon, Vice President, Nuclear Operations
    corrected in a timely manner. Specifically, in February 2006, Susquehanna personnel
T. Gorman, Project Manager, Design Engineering
    identified an incorrect setpoint for the low pressure injection permissive interlock in the
R. Hoffman, Manager, Nuclear Fuels & Analysis
    RHR and CS systems operating procedures and associated hard cards; however, the
    procedures were not revised until July 2007 due to the issue being screened as low
    priority and not a condition adverse to quality (CAQ).
    Description: On February 11, 2006, an AR was written to identify that the low pressure
    injection permissive setpoint in the RHR and CS operating procedures, and the
    associated operator hard cards, was incorrect. The correct setpoint is 420 pounds per
    square inch gage (psig), but the procedures still had the previous setpoint of 436 psig.
    The setpoint had been changed in 1999 as part of a modification. The procedures were
    not revised until July 16, 2007, 17 months after the deficiency was identified in an AR. In
    addition, the inspectors noted that the setpoint in the procedures (436 psig) was not
    within the allowable tolerance (407-433 psig) listed in the Susquehanna TS, Section
    3.3.5.1, Emergency Core Cooling System (ECCS) Instrumentation.
    When the AR was initiated, it was sub-classified as AR/CPG/OPS; that is, assigned to
    the Central Procedures Group and identified as an Operations procedure. It was not
    recognized that deficient operating procedures for safety-related systems may be a CAQ
    and that the AR should have been classified as a Condition Report. The affected
    section in the procedures was the verification of the response of the systems to an
    automatic initiation signal. For example, the Unit 1 RHR procedure OP-149-001, RHR
    System, Section 2.2, noted that No operator action is required unless an automatic
    action failed to occur ... At 436 psig decreasing Reactor pressure, RHR INJ OB ISO
    [injection outboard isolation] HV-151-F015A & B OPEN. If the valves did not open at
    the specified pressure in the procedure and hard card, the operator may have diverted
    their attention unnecessarily and attempted to open the valve manually, even though the
                                                                                            Enclosure


B. McKinney, Chief Nuclear Officer I. Missien, Project Manager, System Engineering B. O'Rourke, Senior Engineer, Nuclear Regulatory Affairs
                                          16
R. Pagodin, General Manager, Nuclear Engineering
interlock would not have been satisfied (420 psig) and the valve would not open in
accordance with the plant design.
The pressure switches were changed in 1999, as part of a Unit 1 plant modification
(Design Change Package (DCP) 97-9075); Unit 2 switches were changed by DCP
97-9076. The modification replaced the existing pressure switches with Barton pressure
indicating switches, because of improved accuracy. The low pressure injection
permissive interlock prevents the CS and RHR injection valves from opening until
reactor pressure has decreased to the RHR and CS systems design pressure, to
prevent over pressurization of the RHR and CS systems. The DCP identified the
specific RHR and CS operating procedures as needing to be changed. Immediate
corrective actions included the initiation of a new CR to evaluate the other pending
procedure changes to determine if their priority should be revised.
The performance deficiency involved a failure to identify and correct a CAQ, the
incorrect setpoint, in a timely manner commensurate with its safety significance. The
inspectors concluded this action was untimely because the modification process would
have revised these procedures prior to the modification being accepted by operations
personnel.
Analysis: The performance deficiency is more than minor because it is associated with
the Procedure Quality attribute of the Mitigating Systems cornerstone and affects the
objective to ensure the availability, reliability, and capability of systems that respond to
initiating events to prevent undesirable consequences. Specifically, the incorrect
setpoint reference in the procedure impacted the reliability of operator response to the
event in that it could delay operator actions or result in misoperation of equipment. The
inspectors performed a review of the finding in accordance with NRC Inspection Manual
Chapter (IMC) 0609, Significance Determination Process (SDP), Attachment 4, Phase
1 - Initial Screening and Characterization of Findings. The inspectors determined that
the finding screened out as having very low safety significance (Green), because it was
not a design deficiency, did not result in an actual loss of safety function, and did not
screen as potentially risk significant due to external initiating events
This performance deficiency has a Cross-Cutting aspect in the area of PI&R, CAP,
because Susquehanna did not identify that a setpoint error in operating procedures for
safety-related systems was a CAQ, commensurate with its safety significance. [P.1(a)]
Enforcement: 10 CFR 50, Appendix B, Criterion XVI, Corrective Action, states, in part,
that conditions adverse to quality shall be promptly identified and corrected. Contrary to
the above, from 1999, when the pressure switches were replaced and the setpoint was
changed, until 2006, when AR 751412 was written, Susquehanna had failed to identify
that the setpoint was wrong for the low pressure injection permissive interlock in the
operating procedures for RHR and CS. Subsequently, on February 11, 2006, when
Susquehanna personnel initiated and approved AR 751412, they failed to identify that
the stated deficiency was a CAQ, which resulted in untimely corrective actions.
Susquehanna considered this to be a procedure change and not a CAQ, and classified
the AR as a CPG versus a CR. As such, the procedures were not changed until July 16,
                                                                                      Enclosure


R. Paley, General Manager, Plant Support
                                                17
    2007, 17 months after the condition was identified and eight years after the setpoint was
    changed in the plant. Because this finding is of very low safety significance (Green), and
    was entered into the Susquehanna CAP (AR/CR 956917) this violation is being treated
    as a Non-Cited Violation (NCV) consistent with Section VI.A.1 of the NRC Enforcement
    Policy.
    (NCV 05000387/2008006-04; 05000388/2008006-04 - Failure to Identify and Correct
    a Setpoint Error in the RHR and CS Operating Procedures)
b.  Assessment of the Use of Operating Experience
1. Inspection Scope
    The team reviewed a sample of operating experience (OE) issues for applicability to
    Susquehanna, and for the associated actions. The documents were reviewed to ensure
    that underlying problems associated with the issues were appropriately considered for
    resolution. The team also reviewed how Susquehanna considered OE for applicability in
    causal evaluations.
    Prior to the start of the inspection, the inspectors noted a potential negative trend in the
    number of issues associated with reactivity management. In accordance with the
    Inspection Procedure, the inspectors increased the scope of the review to determine if
    there was an adverse trend in the area of reactivity management over the past five
    years. The inspectors reviewed select ARs and CRs associated with the control rod
    drive system, control rod problems, human performance issues, and the spent fuel pool;
    the inspectors review included how Susquehanna had incorporated applicable OE for
    these specific systems and human performance issues into the CAP. The inspectors
    interviewed selected licensee staff.
2. Assessment
    In general, OE was effectively used at the station. The inspectors noted that OE was
    reviewed during the causal evaluation process and incorporated, as appropriate, into the
    development of the associated corrective actions. The inspectors noted that OE was
    frequently used in work packages and pre-job briefs. The team did not identify any
    significant deficiencies within the sample reviewed. The team did not identify a negative
    trend nor any significant problems with the control of activities associated with reactivity
    management.
3. Findings
    No findings of significance were identified in the area of operating experience.
c.  Assessment of Self-Assessments and Audits
1. Inspection Scope
                                                                                        Enclosure


A. Price, Supervisor, Corrective Action & Assessment M. Rochester, Employee Concerns Representative G. Ruppert, Manager, Maintenance
                                              18
    The team reviewed a sample of departmental self-assessments, CAP trend reports, and
    Quality Assurance (QA) audits, including QAs most recent audit of the CAP. The team
    also reviewed the latest internal assessment of the safety culture at Susquehanna,
    conducted in October 2006. The reviews were performed to determine if problems
    identified through these evaluations were entered into the CAP system, and whether the
    corrective actions were properly completed to resolve the deficiencies. The
    effectiveness of the audits and self-assessments was evaluated by comparing audit and
    self-assessment results against self-revealing and NRC-identified findings, and
    observations during the inspection.
2. Assessment
    The team considered the quality of the audits and self-assessments to be thorough and
    critical. ARs were initiated for issues identified by QA and the self-assessments. The
    Susquehanna 2006 Comprehensive Cultural Assessment Report consisted of a safety
    culture survey and interviews. The cultural assessment report identified some
    weaknesses at the station, which were entered into the CAP. The team did not identify
    any results that were inconsistent with Susquehannas conclusions.
3. Findings
    No findings of significance were identified in the area of audits and self-assessments.
d.  Assessment of Safety Conscious Work Environment
1. Inspection Scope
    To evaluate the safety conscious work environment (SCWE) at Susquehanna, during
    interviews and discussions with station personnel, the team assessed the workers
    willingness to enter issues into the CAP and to raise safety issues to their management
    and/or to the NRC. The inspectors also interviewed the Employee Concerns Program
    (ECP) representative to determine if employees were aware of the program and had
    used it to raise concerns. The team reviewed a sample of the ECP files to ensure that
    issues were entered into the corrective action program, as appropriate.
2. Assessment
    Based on interviews, observations of plant activities, and reviews of the ARs and ECP,
    the inspectors determined that the site personnel were willing to raise safety issues and
    document them in ARs. Individuals actively utilized the AR system, as evidenced by the
    number and significance of issues entered into the program. The inspectors noted that
    ARs were written by a variety of personnel, from workers to managers. ECP evaluations
    were thorough and appropriate actions were taken to address issues.
3. Findings
    No findings of significance were identified related to the SCWE at Susquehanna.
                                                                                      Enclosure


R. Schechterly, Operating Experience Coordinator
                                            19
4OA6 Meetings, Including Exit:
    On February 1, 2008, the team presented the inspection results to Mr. B. McKinney,
    Senior Vice President, and to other members of the Susquehanna staff, who
    acknowledged the findings. The team confirmed that no proprietary information
    reviewed during the inspection was retained.
ATTACHMENT: Supplemental Information
    In addition to the documentation that the team reviewed (listed in the Attachment),
    copies of information requests given to the licensee are in ADAMS, under accession
    number ML080430585.
                                                                                      Enclosure


R. Sgarro, Manager, Nuclear Regulatory Affairs  
                                                  A-1
M. Sleigh, Security Manager  
                        ATTACHMENT - SUPPLEMENTAL INFORMATION
B. Stitt, Operations Training T. Tonkinson, Supervisor, Maintenance Support D. Weller, Maintenance Foreman  
                                    KEY POINTS OF CONTACT
L. West, Supervisor, Central Procedure Group  
Licensee Personnel:
M. Adelizzi, Risk Engineer
N. DAngelo, Manager, Station Engineering
C. Gannon, Vice President, Nuclear Operations
T. Gorman, Project Manager, Design Engineering
R. Hoffman, Manager, Nuclear Fuels & Analysis
B. McKinney, Chief Nuclear Officer
I. Missien, Project Manager, System Engineering
B. ORourke, Senior Engineer, Nuclear Regulatory Affairs
R. Pagodin, General Manager, Nuclear Engineering
R. Paley, General Manager, Plant Support
A. Price, Supervisor, Corrective Action & Assessment
M. Rochester, Employee Concerns Representative
G. Ruppert, Manager, Maintenance
R. Schechterly, Operating Experience Coordinator
R. Sgarro, Manager, Nuclear Regulatory Affairs
M. Sleigh, Security Manager
B. Stitt, Operations Training
T. Tonkinson, Supervisor, Maintenance Support
D. Weller, Maintenance Foreman
L. West, Supervisor, Central Procedure Group
Nuclear Regulatory Commission:
M. Gray, Branch Chief, Technical Support & Assessment
F. Jaxheimer, Senior Resident Inspector
                      LIST OF ITEMS OPENED, CLOSED, AND DISCUSSED
Opened and Closed:
05000387/2008006-01 NCV Failure to Adequately Evaluate a Deviation from BWROG EPG/SAG
05000388/2008006-01          Resulted in an Inadequate EOP                      (Section 4OA2.a.3 (a))
05000387/2008006-02 NCV      Failure to Identify and Correct Inconsistencies in the Licensing Basis
05000388/2008006-02          and the EOPs                                        (Section 4OA2.a.3 (b))
05000387/2008006-03 NCV Failure to Accurately Model the Simulator for RPV Water Level
05000388/2008006-03          Instrumentation                                    (Section 4OA2.a.3 (c))
05000387/2008006-04 NCV Failure to Identify and Correct a Setpoint Error in the RHR and CS
05000388/2008006-04          Operating Procedures                                (Section 4OA2.a.3 (d))
                                                                                            Attachment


Nuclear Regulatory Commission
                                            A-2
: M. Gray, Branch Chief, Technical Support & Assessment  
                            LIST OF DOCUMENTS REVIEWED
F. Jaxheimer, Senior Resident Inspector
Procedures:
BWROG EGP/SAG and Appendix B Bases, Revision 2
Design Considerations Applicability Sheet Number 42, Emergency Plan, Revision 1
EO-000-102, RPV Control, Revision 2
EO-000-114-1, RPV Flooding, Revision 5
EO-100-103-1, Primary Containment Control, Revision 9
EP-AD-014, Surveillance Testing of Emergency Communications Equipment, Revision 10
EP-AD-015, Review, Revision, and distribution of the SSES Emergency Plan, Revision 11
ME-0RF-161, Control of Fuel Pool Cleanout Activities, Revision 5
ME-0RF-163, Fuel Pool Cleanout - Energy Solutions - Dose Rate Profiling of Irradiated
  Hardware and Liners, Revision 4
MFP-QA-1220, Engineering Change Process Handbook, Revision 2
MI-VL-009, Operation of Leak Rate Monitors, Surge Tank Assemblies and 1035 psig Test
  Pumps, Revision 3
MT-AD-504, Scaffold Erection, Review and Inspection, Revisions 9 & 10
MT-GM-018, Freeze Sealing of Piping, Revision 15
MT-GM-050, Limitorque Type SMB-000 through SMB-4 Operator Maintenance, Revision 12
NASP-QA-202, Independent Technical Review Program, Revision 2
NASP-QA-401, Internal Audits, Revision 9
NASP-QA-700, Performance Assessment Process, Revision 0
NDAP-00-0109, Employee Concerns Program, Revision 10
NDAP-00-0708, Corrective Action Review Board, Revision 4
NDAP-00-0710, Station Trending Program, Revision 1
NDAP-00-0745, Self-Assessment, Benchmarking and Performance Indicators, Revision 7
NDAP-00-0751, Significant Operating Experience Report (SOER) Review Program, Revision 3
NDAP-00-0752, Cause Analysis, Revisions 3 and 4
NDAP-00-0753, Common Issue Analysis, Revision 0
NDAP-00-0778, Performance Improvement Program, Revision 2
NDAP-QA-0103, Audit Program, Revision 9
NDAP-QA-0330, PSTG and Emergency Procedures, Revision 8
NDAP-QA-0330, Symptom Oriented EOP and EP-DS Program and Writers Guide, Revision 3
NDAP-QA-0412, Leakage Rate Test Program, Revision 10
NDAP-QA-0702, Action Request and Condition Report Process, Revision 20
NDAP-QA-0703, Operability Assessments and Requests for Enforcement Discretion,
  Revision 12
NDAP-QA-0720, Station Report Matrix and Reportability Evaluation Guidance, Revision 13
NDAP-QA-0725, Operating Experience Review Program, Revision 11
NDAP-QA-0726, 10CFR50.59 and 10CFR72.48 Implementation, Revision 10
NDAP-QA-1220, Engineering Change Process, Revision 2
NTP-QA-53.1, Susquehanna Fire Brigade Training Program, Revision 15
ODCM-QA-001, ODCM Introduction, Revision 3
ODCM-QA-002, ODCM Review and Revision Control, Revision 4
ODCM-QA-003, Effluent Monitor Setpoints, Revision 3
ODCM-QA-004, Airborne Effluent Dose Calculations, Revision 4
ODCM-QA-005, Waterborne Effluent Dose Calculation, Revision 3
                                                                                    Attachment


LIST OF ITEMS OPENED, CLOSED, AND DISCUSSED
                                                  A-3
  Opened and Closed
ODCM-QA-006, Total Dose Calculation, Revision 2
:  05000387/2008006-01
ODCM-QA-007, Radioactive Waste Treatment Systems, Revision 2
05000388/2008006-01
ODCM-QA-008, Radiological Environmental Monitoring Program, Revision 11
NCV Failure to Adequately Evaluate a Deviation from BWROG EPG/SAG Resulted in an Inadequate EOP (Section 4OA2.a.3 (a))
ODCM-QA-009, Dose Assessment Policy Statements, Revision 2
05000387/2008006-02
ON-145-004, RPV Water Level Anomaly, Revision 13
05000388/2008006-02
OP-024-001, Diesel Generators, Revision 49
NCV Failure to Identify and Correct Inconsistencies in the Licensing Basis
OP-024-004, Transfer and Test Mode Operations of Diesel Generator E, Revision 26
and the EOPs (Section 4OA2.a.3 (b))
OP-149-001, RHR System, Revisions 31 and 32
05000387/2008006-03
OP-151-001, Core Spray System, Revisions 27 & 28
05000388/2008006-03
SE-124-007, Unit 1 Division 1 Diesel Generator LOCA LOOP Test, Revision 15
NCV Failure to Accurately Model the Simulator for RPV Water Level
SE-259-044, LLRT of RHR Containment Spray Penetration Number X-39A, Revision 11
Instrumentation (Section 4OA2.a.3 (c))
SOP-054-B03, Quarterly ESW Flow Verification Loop B, Revision 7
05000387/2008006-04
SSES-EPG, SSES Plant Specific Technical Guideline, Revision 9
05000388/2008006-04
Audits:
NCV Failure to Identify and Correct a Setpoint Error in the RHR and CS
666178, Corrective Action, November 2006 - February 2007
Operating Procedures (Section 4OA2.a.3 (d))   
667966, QA Internal Audit Report, Fuel Management, Revision 0
  Attachment
691277, QA Internal Audit Report Access Authorization and Fitness for Duty, Revision 0
A-2LIST OF DOCUMENTS REVIEWED
706249, Operations Training and Qualification Programs, May - June 2007
  Procedures
718607, QA Internal Audit Report, Engineering, Revision 0
:  BWROG EGP/SAG and Appendix B Bases, Revision 2
744333, Operations, November - December 2007
Design Considerations Applicability Sheet Number 42, Emergency Plan, Revision 1 EO-000-102, RPV Control, Revision 2
792034, QA Internal Audit Report, Security, Revision 0
EO-000-114-1, RPV Flooding, Revision 5 EO-100-103-1, Primary Containment Control, Revision 9 EP-AD-014, Surveillance Testing of Emergency Communications Equipment, Revision 10 EP-AD-015, Review, Revision, and distribution of the SSES Emergency Plan, Revision 11
NEIP Audit of Susquehanna Quality Assurance, June 2006
ME-0RF-161, Control of Fuel Pool Cleanout Activities, Revision 5
Self-Assessments:
ME-0RF-163, Fuel Pool Cleanout - Energy Solutions - Dose Rate Profiling of Irradiated Hardware and Liners, Revision 4 MFP-QA-1220, Engineering Change Process Handbook, Revision 2 MI-VL-009, Operation of Leak Rate Monitors, Surge Tank Assemblies and 1035 psig Test Pumps, Revision 3 MT-AD-504, Scaffold Erection, Review and Inspection, Revisions 9 & 10
2006 Comprehensive Cultural Assessment, September - October 2006
MT-GM-018, Freeze Sealing of Piping, Revision 15 MT-GM-050, Limitorque Type SMB-000 through SMB-4 Operator Maintenance, Revision 12 NASP-QA-202, Independent Technical Review Program, Revision 2
CA&A Functional Unit Excellence Plan, 1st, 2nd, and 3rd Quarters 2007
NASP-QA-401, Internal Audits, Revision 9
CAA-06-01, Site Wide Self-Assessment, December 2006
NASP-QA-700, Performance Assessment Process, Revision 0
CAA-06-05, Self-Assessment Program Performance, February 2006
NDAP-00-0109, Employee Concerns Program, Revision 10
CAA-06-08, Decrease in CR Generation Identified by Trend Report, November 2006
NDAP-00-0708, Corrective Action Review Board, Revision 4 NDAP-00-0710, Station Trending Program, Revision 1 NDAP-00-0745, Self-Assessment, Benchmarking and Performance Indicators, Revision 7
Focused Self Assessment, MOV Program Self-Assessment, October 2007
NDAP-00-0751, Significant Operating Experience Report (SOER) Review Program, Revision 3  
Maintenance Implementing Procedures Adequacy for Qualified, Inexperienced Employees,
NDAP-00-0752, Cause Analysis, Revisions 3 and 4
  June 2007
NDAP-00-0753, Common Issue Analysis, Revision 0 NDAP-00-0778, Performance Improvement Program, Revision 2 NDAP-QA-0103, Audit Program, Revision 9
Multi-Utility Joint Audit Program Initiative, March - April 2007
NDAP-QA-0330, PSTG and Emergency Procedures, Revision 8
NTG Focused Self-Assessment of Operator Training Programs, June 2007
NDAP-QA-0330, Symptom Oriented EOP and EP-DS Program and Writer's Guide, Revision 3 NDAP-QA-0412, Leakage Rate Test Program, Revision 10
OPS-06-02, Determine the Status of Operator Fundamentals, February 2006
NDAP-QA-0702, Action Request and Condition Report Process, Revision 20 NDAP-QA-0703, Operability Assessments and Requests for Enforcement Discretion, Revision 12 NDAP-QA-0720, Station Report Matrix and Repor
OPS-06-03, Operations Focused Se-f Assessment, July 2006
tability Evaluation Guidance, Revision 13 NDAP-QA-0725, Operating Experience Review Program, Revision 11
Pre-PI&R Focused Self-Assessment, September 2007
NDAP-QA-0726, 10CFR50.59 and 10CFR72.48 Implementation, Revision 10 NDAP-QA-1220, Engineering Change Process, Revision 2 NTP-QA-53.1, Susquehanna Fire Brigade Training Program, Revision 15
QA Organization Effectiveness Self-Assessment, October 2006
ODCM-QA-001, ODCM Introduction, Revision 3
QA-06-01, Operations QA Audit Preparation Gap Analysis for QC, May - July 2006
ODCM-QA-002, ODCM Review and Revision Control, Revision 4
SEC-06-01, Analyses of SSES Security Procedures and Physical Security Plan, Revision 0
ODCM-QA-003, Effluent Monitor Setpoints, Revision 3 ODCM-QA-004, Airborne Effluent Dose Calculations, Revision 4
                                                                                    Attachment
ODCM-QA-005, Waterborne Effluent Dose Calculation, Revision 3 
  Attachment
A-3ODCM-QA-006, Total Dose Calculation, Revision 2  
ODCM-QA-007, Radioactive Waste  
Treatment Systems, Revision 2  
ODCM-QA-008, Radiological Environmental Monitoring Program, Revision 11 ODCM-QA-009, Dose Assessment Policy Statements, Revision 2 ON-145-004, RPV Water Level Anomaly, Revision 13  
OP-024-001, Diesel Generators, Revision 49  
OP-024-004, Transfer and Test Mode Operations of Diesel Generator E, Revision 26  
OP-149-001, RHR System, Revisions 31 and 32 OP-151-001, Core Spray System, Revisions 27 & 28 SE-124-007, Unit 1 Division 1 Diesel Generator LOCA LOOP Test, Revision 15  
SE-259-044, LLRT of RHR Containment Spray Penetration Number X-39A, Revision 11  
SOP-054-B03, Quarterly ESW Flow Verification Loop B, Revision 7  
SSES-EPG, SSES Plant Specific Technical Guideline, Revision 9  


   
                                        A-4
Audits: 666178, Corrective Action, November 2006 - February 2007
Action Requests (* denotes an AR/CR generated as a result of this inspection):
667966, QA Internal Audit Report, Fuel Management, Revision 0
478369  724467  741707  759209  779830  810391  843985    873741  896685  941677
691277, QA Internal Audit Report Access Authorization and Fitness for Duty, Revision 0 706249, Operations Training and Qualification Programs, May - June 2007 718607, QA Internal Audit Report, Engineering, Revision 0
524893  724717  741908  759216  780144  810513  845441    873919  897250  941810
744333, Operations, November - December 2007
542157  726672  741943  759827  780155  811239  849935    874227  898909  947160
792034, QA Internal Audit Report, Security, Revision 0
545804  728295  742191  760281  780778  811429  851918    875597  899429  954950*
NEIP Audit of Susquehanna Quality Assurance, June 2006
549328  728936  742318  760526  780992  811996  853358    875976  900301  954970*
554362  730852  742342  760526  781644  812948  854681    876021  900720  954972*
554598  730944  742427  762497  782321  813844  855266    876427  901262  954975*
555140  730947  742676  763050  782344  815268  855268    877419  903439  954990*
555263  737236  742966  763128  783655  816097  856997    877727  904689  955072*
555562  738555  743043  763397  784730  816710  858269    877743  908163  955073*
557348  738575  744975  764145  784882  817720  858578    878165  911601  955111*
565795  738634  744979  764738  784890  818082  859082    878326  912213  955130*
575128  738653  745221  764953  785561  818154  859440    879080  912476  955150*
578943  738907  745248  765421  785791  820344  859794    879847  915167  955151*
584400  738999  745462  767566  786149  820380  859839    880331  915620  955761*
591033  739262  745773  767567 786224  820989  860299    880573  916453  955780*
594366  739371  746658  768301  786564  820995  860551    880702  916463  956339*
594887  739371  747077  768502  786735  821006  861162    880806  916873  956344*
595165  739386  747438  768821  786768  821064  861366    881210  917196  956431*
604009  739419  749294  768920  787850  822996  861415    881219  918392  956696*
604296  739579  749341  769304  788616  823908  862474    881225  918549  956914*
610978  739625  749832  769867  788621  824522  864090    881236  919470  956917*
615707  739713  750140  769870  788879  824895  865286    882318  927046  957319*
623914  739737  750232  770453  789971  825107  865423    883987  928515  957484*
623949  740043  751212  771319  791115  825750  865804    886209  929461  957637*
635924  740073  751412  771876  791329  826452  865924    887048  930075  958769*
647827  740303  751433  771961  792158  826870  866930    887067  930571  959670*
655735  740477  751444  773046  793381  827023  867534    888310  931113  961655
666405  740538  752341  773409  794995  827966  867747    889683  932590  962390
668871  740658  752347  774453  795583  828626  867881    889966  936060  962881*
669732  740668  752582  774475  796640  828744  868251    891288  936250  963061*
677145  740723  753392  774509  797517  829065  868259    891733  936370  963065*
687080  740802  753664  774549  799890  829502  868828    891795  936631  963698*
688300  740804  753869  775285  802254  835002  868874    892142  937123  963861*
691108  740825  753990  775718  802539  837153  869819    892152  938054  964512*
693936  740946  755360  776112  802563  837180  869824    892528  938698  964514*
699781  740948  756094  776171  802572  839753  870968    893090  938722  964836*
723483  740955  756415  776769  802697  841169  871013    893157  939516 965167*
723976  740988  756804  776918  805698  841885  872039    893290  939780
724102 741041  757530  777335  806710  842663  872056    895147  941290
724165  741321  757979  777723  809503  842920  873026    896455  941401
724374  741457  758337  778124  809702  843144  873683    896505  941626
                                                                              Attachment


                                              A-5
Self-Assessments
Maintenance Work Requests (SPWO):
: 2006 Comprehensive Cultural Assessment, September - October 2006
099065        099364        766396      766413        767284      768234      862569
CA&A Functional Unit Excellence Plan, 1
099115        448229        766401      766416        767490      768618      862578
st , 2 nd , and 3 rd Quarters 2007 CAA-06-01, Site Wide Self-Assessment, December 2006 CAA-06-05, Self-Assessment Program Performance, February 2006 CAA-06-08, Decrease in CR Generation Identified by Trend Report, November 2006
099120        473889        766406      766496        767506      818282      866262
Focused Self Assessment, MOV Program Self-Assessment, October 2007
099259        570758        766411      767283        767532      862503      866284
Maintenance Implementing Procedures Adequacy
Non-Cited Violations and Findings Reviewed:
for Qualified, Inexperienced Employees, June 2007 Multi-Utility Joint Audit Program Initiative, March - April 2007
NCV 2005005-01, Inadequate FME Exclusion Procedural Instructions Associated with EDG
NTG Focused Self-Assessment of Operator Training Programs, June 2007 OPS-06-02, Determine the Status of Operator Fundamentals, February 2006
    Work
OPS-06-03, Operations Focused Se-f Assessment, July 2006
FIN 2005009-01, Fire Brigade Drill Program Not Consistent with Regulatory Guidance and
Pre-PI&R Focused Self-Assessment, September 2007
    Industry Standards
QA Organization Effectiveness Self-Assessment, October 2006 QA-06-01, Operations QA Audit Preparation Gap Analysis for QC, May - July 2006 SEC-06-01, Analyses of SSES Security Procedures and Physical Security Plan, Revision 0
NCV 2006002-01, Equipment Hatch Plugs are Not Watertight as Indicated in FSAR
FIN 2006002-02, Incomplete Corrective Actions Contribute to CRD Flow Control Failure
NCV 2006003-01, Inadequate Procedures Resulted in Motor Operated Valve Failures
NCV 2006003-02, Failure to Identify Material Degradation which Resulted in the Failure of the
    C ESW Pump Breaker
NCV 2006003-03, Inadequate Procedure Results in Elevated Reactor Coolant System Leakage
NCV 2006003-04, Inadequate Design Review of PRDNMS Modification Resulted in a Reactor
    Scram
NCV 2006003-05, Ineffective Corrective Actions to Assure Training and Qualification of Workers
    as Required by 10CFR50, Appendix B, Criterion XVI
NCV 2006004-01, Inadequate Risk Assessment
NCV 2006005-01, Inadequate Work Instructions for the Disassembly and Inspection of Check
    Valves
NCV 2006005-02, Inadequate Evaluation of EPA Breaker Failures
NCV 2006006-01, Failure to Identify Scaffolding that Affected the Safety-Related RHR
    Discharge Pressure Instrument Tubing Input to ADS
NCV 2006009-01, Safeguards Information
Licensee Identified NCV 2007002, U2 Div II Core Spray Pump Room (a High Radiation Area)
    Was Not Posted and Was Open
Licensee Identified NCV 2007002, U1 HPCI Failed a Surveillance Due to the Failure to Perform
    Preventive Maintenance
NCV 2007003-01, Failure to Take Timely Corrective Actions for an E EDG Jacket Water Leak
FIN 2007003-02, Failure to Maintain Occupational Radiation Exposure ALARA during Reactor
    Water Cleanup Pipe Replacement Activities
FIN 2007003-03, Failure to Maintain Occupational Radiation Exposure ALARA during Outage
    ISI of Reactor Pressure Vessel
NCV 2007003-04, Violation of 10CFR71.5 for Inadequately Secured Transport of Condensate
    Pump Motors
NCV 2007003-05, Violation of 10CFR71.5 for Inadequately Accounting for Activity in a
    Shipment of Irradiated Fuel Channels
Licensee Identified NCV 2007003, U2 Reactor Building HRA Postings and Boundary Moved
    without Permission of RP
NCV 2007007-01, Inoperable ESSW Pump-House Ventilation Lineup
NCV 2007007-02, Failure to Use E EDG Procedure
                                                                                      Attachment


                                              A-6
Miscellaneous:
   
5059-01-2356, 50.59 Screen of Specification C-1056, Long Term Scaffolding, Revision 4
  Attachment
CP067, Corrective Action Program - Evaluation & Resolution, Revision 8
A-4Action Requests (* denotes an AR/CR generated as a result of this inspection)
    (Lesson Plan & Student Material)
: 478369 524893 542157
CP068, Managing the Corrective Action Process, Revision 2 (Lesson Plan & Student Material)
545804
Daily CR Screening Team Package
549328
Design Verification Checklist for SCN 6 for Specification C-1056, dated April 27, 2001
554362 554598 555140
EC-059-1024, Design Requirements for and Evaluation of Potential Secondary Containment
555263
    Bypass Leakage Pathways, Revision 4
555562
EC-RADN-1029, SSES Design Basis LOCA Dose Consequence Evaluation for Containment
557348
    Bypass Leakage Including the Effects of Suppression Pool Scrubbing, Revision 1
565795 575128 578943
EC-SIMU-1001, Evaluation of Simulator Level Instrument Response to Large LOCA, dated
584400
    May 4, 1994
591033
Engineering Specification C-1056, Erection of Scaffolding in Safety-Related Areas, Revision 4
594366 594887 595165
EWR #MIS-85-0460, Design Inputs and Considerations Checklist for Specification C-1056,
604009
    Revision 2
604296
Hot Box Item 08-01, Reactor Water Instrumentation Response during DBA LOCA, dated
610978
    January 31, 2008
615707 623914 623949
IEEE Standard 497-2002, IEEE Standard Criteria for Accident Monitoring Instrumentation, dated
635924
    September 30, 2002
647827
Long Term Scaffold Log, dated January 16, 2008
655735 666405 668871
No Degraded Condition Response to OFR 963310, dated January 30, 2008
669732
NRC Information Notice 2007-29, Temporary Scaffolding Affects Operability of Safety-Related
677145
    Equipment, dated September 17, 2007
687080
NRC Inspection Procedure 42001, Emergency Operating Procedures, dated June 28, 1991
688300 691108 693936
NRC Regulatory Guide 1.97, Instrumentation for Light-Water-Cooled Nuclear Power Plants to
699781
    Assess Plant and Environs Conditions During and Following an Accident, Revision 2
723483
NRC Regulatory Issue Summary 2005-20, Information to Licensees Regarding Two NRC
723976 724102 724165
    Inspection Manual Sections on Resolution of Degraded and Nonconforming Conditions and
724374 724467 724717 726672
    on Operability
728295
NRC Regulatory Issue Summary 2007-21, Adherence to Licensed Power Limits, dated
728936
    August 23, 2007
730852 730944 730947
NEDE-24801, Review of BWR Reactor Vessel Water Level Measurement, April 1980
737236
NEDO-24708A, Additional Information Required for NRC Staff Generic Report on Boiling Water
738555
    Reactors, Revision 1
738575
Operational Policy Statement (OPS) - 5, Deficiency Control System, Revision 13
738634 738653 738907
Operations Monthly Performance Indicators, December 2007
738999
Operations Quality Assurance Manual, dated December 13, 2007
739262
OPEX Daily Report, January 29, 2008
739371 739371 739386
Plant Modification Package - DCP/ECO #97-9075, Unit 1 Core Spray/RHR/LPCI Pressure
739419
    Switch Replacement, Revision 1
739579
PL-NF-02-07, Channel Management Action Plan, Revision 28
739625
Regulatory Guide 1.97, Criteria for Accident Monitoring Instrumentation, Revision 4
739713 739737 740043
Specification Change Notice #6 for C-1056, Revision 3
740073
Temporary Scaffold Log, dated January 15, 2008
740303
Unit 1 & 2, Control Rod Drive Hydraulics System Health Report, May - August 2007
740477 740538 740658
Unit 1, RHR Residual Heat Removal System Health Report, September - December 2007
740668
                                                                                      Attachment
740723
740802
740804 740825 740946
740948
740955
740988 741041 741321
741457 741707 741908 741943
742191
742318
742342 742427 742676
742966
743043
744975
744979 745221 745248
745462
745773
746658 747077 747438
749294
749341
749832
750140 750232 751212
751412
751433
751444 752341 752347
752582
753392
753664
753869 753990 755360
756094
756415
756804 757530 757979
758337 759209 759216 759827
760281
760526
760526 762497 763050
763128
763397
764145
764738 764953 765421
767566
767567
768301 768502 768821
768920
769304
769867
769870 770453 771319
771876
771961
773046 773409 774453
774475
774509
774549
775285 775718 776112
776171
776769
776918 777335 777723
778124 779830 780144 780155
780778
780992
781644 782321 782344
783655
784730
784882
784890 785561 785791
786149
786224
786564 786735 786768
787850
788616
788621
788879 789971 791115
791329
792158
793381 794995 795583
796640
797517
799890
802254 802539 802563
802572
802697
805698 806710 809503
809702 810391 810513 811239
811429
811996
812948 813844 815268
816097
816710
817720
818082 818154 820344
820380
820989
820995 821006 821064
822996
823908
824522
824895 825107 825750
826452
826870
827023 827966 828626
828744
829065
829502
835002 837153 837180 839753
841169
841885 842663 842920
843144 843985 845441 849935
851918
853358
854681 855266 855268
856997
858269
858578
859082 859440 859794
859839
860299
860551 861162 861366
861415
862474
864090
865286 865423 865804
865924
866930
867534 867747 867881
868251
868259
868828
868874 869819 869824
870968
871013
872039 872056 873026
873683 873741 873919 874227
875597
875976
876021 876427 877419
877727
877743
878165
878326 879080 879847
880331
880573
880702 880806 881210
881219
881225
881236
882318 883987 886209
887048
887067
888310 889683 889966
891288
891733
891795
892142 892152 892528
893090
893157
893290 895147 896455
896505 896685 897250 898909
899429
900301
900720 901262 903439
904689
908163
911601
912213 912476 915167
915620
916453
916463 916873 917196
918392
918549
919470
927046 928515 929461
930075
930571
931113 932590 936060
936250
936370
936631
937123 938054 938698
938722
939516
939780 941290 941401
941626 941677 941810 947160
954950*
954970*
954972* 954975* 954990*
955072*
955073*
955111*
955130* 955150* 955151*
955761*
955780*
956339* 956344* 956431*
956696*
956914*
956917*
957319* 957484* 957637*
958769*
959670*
961655 962390 962881*
963061*
963065*
963698*
963861* 964512* 964514*
964836*
965167*   
  Attachment
A-5 Maintenance Work Requests (SPWO)
:  099065 099115 099120
099259 099364 448229 473889
570758 766396 766401 766406
766411 766413 766416 766496
767283 767284 767490 767506
767532 768234 768618 818282
862503 862569 862578 866262
866284  Non-Cited Violations and Findings Reviewed
:  NCV 2005005-01, Inadequate FME Exclusion Procedural Instructions Associated with EDG
Work FIN 2005009-01, Fire Brigade Drill Program Not Consistent with Regulatory Guidance and
Industry Standards NCV 2006002-01, Equipment Hatch Plugs are Not Watertight as Indicated in FSAR FIN 2006002-02, Incomplete Corrective Actions Contribute to CRD Flow Control Failure NCV 2006003-01, Inadequate Procedures Resulted in Motor Operated Valve Failures
NCV 2006003-02, Failure to Identify Material Degradation which Resulted in the Failure of the "C" ESW Pump Breaker NCV 2006003-03, Inadequate Procedure Results in Elevated Reactor Coolant System Leakage NCV 2006003-04, Inadequate Design Review of PRDNMS Modification Resulted in a Reactor
Scram NCV 2006003-05, Ineffective Corrective Actions to Assure Training and Qualification of Workers as Required by 10CFR50, Appendix B, Criterion XVI NCV 2006004-01, Inadequate Risk Assessment
NCV 2006005-01, Inadequate Work Instructions for the Disassembly and Inspection of Check
Valves NCV 2006005-02, Inadequate Evaluation of EPA Breaker Failures
NCV 2006006-01, Failure to Identify Scaffolding that Affected the Safety-Related RHR Discharge Pressure Instrument Tubing Input to ADS NCV 2006009-01, Safeguards Information Licensee Identified NCV 2007002, U2 Div II Core Spray Pump Room (a High Radiation Area) Was Not Posted and Was Open Licensee Identified NCV 2007002, U1 HPCI Failed a Surveillance Due to the Failure to Perform
Preventive Maintenance NCV 2007003-01, Failure to Take Timely Corrective Actions for an "E" EDG Jacket Water Leak
FIN 2007003-02, Failure to Maintain Occupational Radiation Exposure ALARA during Reactor
Water Cleanup Pipe Replacement Activities FIN 2007003-03, Failure to Maintain Occupational Radiation Exposure ALARA during Outage ISI of Reactor Pressure Vessel NCV 2007003-04, Violation of 10CFR71.5 for Inadequately Secured Transport of Condensate Pump Motors NCV 2007003-05, Violation of 10CFR71.5 for Inadequately Accounting for Activity in a Shipment of Irradiated Fuel Channels Licensee Identified NCV 2007003, U2 Reactor Building HRA Postings and Boundary Moved
without Permission of RP NCV 2007007-01, Inoperable ESSW Pump-House Ventilation Lineup NCV 2007007-02, Failure to Use "E" EDG Procedure
 
  Attachment
A-6 Miscellaneous
5059-01-2356, 50.59 Screen of Specification C-1056, Long Term Scaffolding, Revision 4 CP067, Corrective Action Program - Evaluation & Resolution, Revision 8 (Lesson Plan & Student Material) CP068, Managing the Corrective Action Process, Revision 2 (Lesson Plan & Student Material)  
Daily CR Screening Team Package  
Design Verification Checklist for SCN 6 for Specification C-1056, dated April 27, 2001 EC-059-1024, Design Requirements for and Evaluation of Potential Secondary Containment  
Bypass Leakage Pathways, Revision 4 EC-RADN-1029, SSES Design Basis LOCA Dose
Consequence Evaluation for Containment Bypass Leakage Including the Effects of Suppression Pool Scrubbing, Revision 1 EC-SIMU-1001, Evaluation of Simulator Level Instrument Response to Large LOCA, dated May 4, 1994 Engineering Specification C-1056, Erection of Scaffolding in Safety-Related Areas, Revision 4 EWR #MIS-85-0460, Design Inputs and Considerations Checklist for Specification C-1056, Revision 2 Hot Box Item 08-01, Reactor Water Instrumentation Response during DBA LOCA, dated  
January 31, 2008 IEEE Standard 497-2002, IEEE Standard Criteria for Accident Monitoring Instrumentation, dated September 30, 2002 Long Term Scaffold Log, dated January 16, 2008  
No Degraded Condition Response to OFR 963310, dated January 30, 2008  
NRC Information Notice 2007-29, Temporary Scaffolding Affects Operability of Safety-Related  
Equipment, dated September 17, 2007 NRC Inspection Procedure 42001, Emergency Operating Procedures, dated June 28, 1991 NRC Regulatory Guide 1.97, Instrumentation for Light-Water-Cooled Nuclear Power Plants to Assess Plant and Environs Conditions During and Following an Accident, Revision 2 NRC Regulatory Issue Summary 2005-20, Information to Licensees Regarding Two NRC Inspection Manual Sections on Resolution of Degraded and Nonconforming Conditions and  
on Operability NRC Regulatory Issue Summary 2007-21, Adherence to Licensed Power Limits, dated August 23, 2007 NEDE-24801, Review of BWR Reactor Vessel Water Level Measurement, April 1980  
NEDO-24708A, Additional Information Required for NRC Staff Generic Report on Boiling Water  
Reactors, Revision 1 Operational Policy Statement (OPS) - 5, Deficiency Control System, Revision 13 Operations Monthly Performance Indicators, December 2007  


Operations Quality Assurance Manual, dated December 13, 2007
                                        A-7
OPEX Daily Report, January 29, 2008
                              LIST OF ACRONYMS
Plant Modification Package - DCP/ECO #97-9075, Unit 1 Core Spray/RHR/LPCI Pressure
ACE     Apparent Cause Evaluation
Switch Replacement, Revision 1 PL-NF-02-07, Channel Management Action Plan, Revision 28
AR     Action Request
Regulatory Guide 1.97, Criteria for Accident Monitoring Instrumentation, Revision 4
BWROG   Boiling Water Reactor Owners Group
Specification Change Notice #6 for C-1056, Revision 3
CAP     Corrective Action Program
Temporary Scaffold Log, dated January 15, 2008 Unit 1 & 2, Control Rod Drive Hydraulics System Health Report, May - August 2007 Unit 1, RHR Residual Heat Removal System Health Report, September - December 2007 
CAQ     Condition Adverse to Quality
  Attachment
CARB   Corrective Action Review Board
A-7LIST OF ACRONYMS
CFR     Code of Federal Regulations
  ACE Apparent Cause Evaluation AR Action Request BWROG Boiling Water Reactor Owners' Group  
CPG     Central Procedure Group
CAP Corrective Action Program  
CR     Condition Report
CAQ Condition Adverse to Quality  
CS     Core Spray
CARB Corrective Action Review Board CFR Code of Federal Regulations CPG Central Procedure Group  
DBA     Design Basis Accident
CR Condition Report  
DCP     Design Change Package
CS Core Spray  
ECCS   Emergency Core Cooling System
DBA Design Basis Accident  
ECP     Employee Concerns Program
DCP Design Change Package ECCS Emergency Core Cooling System ECP Employee Concerns Program  
EOP     Emergency Operating Procedures
EOP Emergency Operating Procedures  
EPG/SAG Emergency Procedure Guidelines / Severe Accident Guidelines
EPG/SAG Emergency Procedure Guidelines / Severe Accident Guidelines EPU Extended Power Uprate FSAR Final Safety Analysis Report IMC NRC Inspection Manual Chapter  
EPU     Extended Power Uprate
LOCA Loss of Coolant Accident  
FSAR   Final Safety Analysis Report
NCV Non-Cited Violation  
IMC     NRC Inspection Manual Chapter
NRC Nuclear Regulatory Commission  
LOCA   Loss of Coolant Accident
OE Operating Experience PAM Post-Accident Monitoring PI&R Problem Identification and Resolution  
NCV     Non-Cited Violation
psig pounds per square inch  
NRC     Nuclear Regulatory Commission
PSTG Plant Specific Technical Guidelines  
OE     Operating Experience
QA Quality Assurance RCA Root Cause Analysis RHR Residual Heat Removal  
PAM     Post-Accident Monitoring
ROP Reactor Oversight Program  
PI&R   Problem Identification and Resolution
RPV Reactor Pressure Vessel  
psig   pounds per square inch
SCWE Safety Conscious Work Environment  
PSTG   Plant Specific Technical Guidelines
SDP Significance Determination Process TS Technical Specifications
QA     Quality Assurance
RCA     Root Cause Analysis
RHR     Residual Heat Removal
ROP     Reactor Oversight Program
RPV     Reactor Pressure Vessel
SCWE   Safety Conscious Work Environment
SDP     Significance Determination Process
TS     Technical Specifications
                                                                    Attachment
}}
}}

Revision as of 18:37, 14 November 2019

IR 05000387-08-006, 05000388-08-006, on 01/14/2008 - 02/01/2008, Susquehanna Steam Electric Station; Biennial Baseline Inspection of He Identification and Resolution of Problems; Corrective Action Program, Simulator Fidelity, and Procedure
ML080770308
Person / Time
Site: Susquehanna  Talen Energy icon.png
Issue date: 03/17/2008
From: Mel Gray
Division Reactor Projects I
To: Mckinney B
Susquehanna
Gray M, RI/DRP/TSAB/610-337-5209
References
IR-08-006
Download: ML080770308 (29)


See also: IR 05000387/2008006

Text

UNITED STATES

NUCLEAR REGULATORY COMMISSION

REGION I

475 ALLENDALE ROAD

KING OF PRUSSIA, PA 19406-1415

March 17, 2008

Mr. Britt T. McKinney

Senior Vice President and Chief Nuclear Officer

PPL Susquehanna, LLC

769 Salem Blvd. - NUCSB3

Berwick, PA 18603-0467

SUBJECT: SUSQUEHANNA STEAM ELECTRIC STATION, UNITS 1 AND 2

PROBLEM IDENTIFICATION AND RESOLUTION INSPECTION

INSPECTION REPORTS NOS. 05000387/2008006; 05000388/2008006

Dear Mr. McKinney:

On February 1, 2008, the US Nuclear Regulatory Commission (NRC) completed a team

inspection at the Susquehanna Steam Electric Station. The enclosed inspection report

documents the inspection results, which were discussed on February 1, 2008, with you and

members of your staff.

This inspection was an examination of activities conducted under your license as they relate to

the identification and resolution of problems, and compliance with the Commission=s rules and

regulations and the conditions of your license. Within these areas, the inspection involved

examination of selected procedures and representative records, observations of activities, and

interviews with personnel.

On the basis of the sample selected for review, the team concluded that the implementation of

the corrective action program (CAP) was adequate in that personnel identified issues at a low

threshold; generally screened and prioritized issues in a timely manner; evaluated the issues

commensurate with their safety significance; and implemented corrective actions in a timely

manner commensurate with the safety significance.

The team identified four findings of very low safety significance (Green). These findings were

determined to involve violations of regulatory requirements. However, because each of the

violations was of very low safety significance (Green) and because they were entered into your

corrective action program, the NRC is treating these as Non-Cited Violations (NCVs), in

accordance with Section VI.A.1 of the NRC=s Enforcement Policy. If you contest any NCV in

this report, you should provide a response within 30 days of the date of this inspection report,

with the basis for your denial, to the U.S. Nuclear Regulatory Commission, ATTN: Document

Control Desk, Washington DC, 20555-0001, with copies to the Regional Administrator, Region I;

B. McKinney 2

the Director, Office of Enforcement, U.S. Nuclear Regulatory Commission, Washington, DC,

20555-0001; and the NRC Resident Inspector at the Susquehanna facility.

In accordance with 10 CFR 2.390 of the NRC=s ARules of Practice,@ a copy of this letter and its

enclosure, and your response (if any), will be available electronically for public inspection in the

NRC Public Document Room or from the Publicly Available Records (PARS) component of the

NRC=s document system (ADAMS). ADAMS is accessible from the NRC Web site at

http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room).

Sincerely,

/RA/

Mel Gray, Chief

Technical Support & Assessment Branch

Division of Reactor Projects

Docket Nos. 50-387, 50-388

License Nos. NPF-14; NPF-22

Enclosure: Inspection Report Nos. 05000387/2008006; 05000388/2008006

w/ Attachment: Supplemental Information

cc w/encl:

C. Gannon, Vice President, Nuclear Operations

R. Paley, General Manager, Plant Support

R. Pagodin, General Manager, Nuclear Engineering

R. Sgarro, Manager, Nuclear Regulatory Affairs

Supervisor, Nuclear Regulatory Affairs

M. Crowthers, Supervising Engineer, Nuclear Regulatory Affairs

R. Peal, Mgr, Training, Susquehanna

Manager, Quality Assurance

J. Scopelliti, Community Relations Manager, Susquehanna

B. Snapp, Esq., Associate General Counsel, PPL Services Corporation

Supervisor - Document Control Services

R. Osborne, Allegheny Electric Cooperative, Inc.

D. Allard, Dir, PA Dept of Environmental Protection

Board of Supervisors, Salem Township

J. Johnsrud, National Energy Committee, Sierra Club

E. Epstein, TMI-Alert (TMIA)

J. Powers, Dir, PA Office of Homeland Security

R. French, Dir, PA Emergency Management Agency

1

U.S. NUCLEAR REGULATORY COMMISSION

REGION I

Docket No: 50-387, 50-388

License No: NPF-14, NPF-22

Report No: 05000387/2008006, 05000388/2008006

Licensee: PPL Susquehanna, LLC

Facility: Susquehanna Steam Electric Station, Units 1 and 2

Location: 769 Salem Boulevard - NUCSB3

Berwick, PA 18603-0467

Dates: January 14 - February 1, 2008

Team Leader: B. Norris, Senior Project Engineer, Division of Reactor Projects

Inspectors: F. Arner, Senior Reactor Inspector, Division of Reactor Safety

R. Fuhrmeister, Senior Project Engineer, Division of Reactor Projects

G. Ottenberg, Resident Inspector, Division of Reactor Projects

J. Bream, Reactor Engineer, Division of Reactor Projects

R. McKinley, Operations Examiner, Division of Reactor Safety

Approved by: Mel Gray, Chief

Technical Support & Assessment Branch

Division of Reactor Projects

Enclosure

2

SUMMARY OF FINDINGS

IR 05000387/2008-006, 05000388/2008-006; 01/14/2008 - 02/01/2008; Susquehanna Steam

Electric Station; Biennial Baseline Inspection of the Identification and Resolution of Problems;

Corrective Action Program, Simulator Fidelity, and Procedure Quality.

This team inspection was performed by five NRC regional inspectors and one resident

inspector. Four findings of very low safety significance (Green) were identified during this

inspection and determined to be Non-Cited Violations (NCVs). The significance of most findings

is indicated by their color (Green, White, Yellow, Red) using NRC Inspection Manual Chapter (IMC) 0609, ASignificance Determination Process@ (SDP). The NRC=s program for overseeing

the safe operation of commercial nuclear power reactors is described in NUREG-1649, AReactor

Oversight Process,@ Revision 4, dated December 2006.

Identification and Resolution of Problems

The team concluded that the implementation of the corrective action program (CAP) at

Susquehanna was adequate in that personnel identified issues at a low threshold and used a

single entry-point system to document the problems by the initiation of an Action Request (AR).

About 20 percent of the ARs were considered to be conditions adverse to quality (CAQ) and

sub-classified as a Condition Report (CR). However, the team identified several ARs that

should have been classified as CAQs; as a result, CRs were not written and corrective actions

were not timely. The team identified two findings of very low significance related to the AR

process that had current performance cross-cutting aspects in problem identification because

the issues were not categorized commensurate with their safety significance. Notwithstanding

these two findings, the team concluded that in general Susquehanna personnel screened and

prioritized CRs in a timely manner using established criteria.

The team also concluded that Susquehanna personnel properly evaluated the issues

commensurate with their safety significance; and generally implemented corrective actions in a

timely manner, commensurate with the safety significance. The team noted that Susquehanna

reviewed and applied industry operating experience lessons learned. Audits and self-

assessments added value to the corrective action process. On the basis of interviews

conducted during the inspection, workers at the site expressed freedom to enter safety

concerns into the CAP.

Enclosure

3

a. NRC Identified and Self-Revealing Findings

Cornerstone: Mitigating Systems

C Green: The NRC identified a Non-Cited Violation of 10 CFR 50, Appendix B, Criterion V,

Instructions, Procedures, and Drawings, because, in the 1990s, Susquehanna failed to

adequately evaluate a deviation from the Boiling Water Reactor Owners Group

Emergency Procedure Guidelines / Severe Accident Guidelines (BWROG EPG/SAG),

which resulted in one of the emergency operating procedures (EOPs) being inadequate.

Specifically, Caution #1 in the BWROG EPG/SAG warned the operators that reactor

pressure vessel (RPV) level instrumentation may be unreliable if the drywell

temperatures exceeded RPV saturation temperature. The purpose of the Caution was

to give the operators a chance to evaluate the validity of the RPV level instrumentation

to avoid premature entry into the RPV flooding contingency procedure. Susquehanna

did not adequately evaluate the deviation, and the Susquehanna EOPs did not use a

Caution statement; but instead, changed the caution to a procedural step, which directed

the operators to transition directly to the RPV flooding procedure.

The performance deficiency is more than minor because it is associated with the

Procedure Quality attribute of the Mitigating Systems cornerstone and affects the

objective to ensure the availability, reliability, and capability of systems that respond to

initiating events to prevent undesirable consequences. Specifically, the EOP could have

directed entry into the RPV flooding procedure unnecessarily which would have

restricted the use of suppression pool cooling and required other actions that would have

complicated the operators response to the event. The finding was determined to be of

very low safety significance because it was not a design deficiency, did not result in an

actual loss of safety function, and did not screen as potentially risk significant due to

external initiating events. (Section 4OA2.a.3 (a))

C Green: The NRC identified a Non-Cited Violation of 10 CFR 50, Appendix B, Criterion

XVI, Corrective Action, for the failure to identify that an inconsistency between the

procedures and the design basis for suppression pool (SP) cooling was a condition

adverse to quality (CAQ), which resulted in corrective actions not being taken in a timely

manner. Specifically, in January 2006, a Condition Report (CR) identified an

inconsistency between an assumption in the Final Safety Analysis Report (FSAR) for the

design basis accident and the emergency operating procedures (EOPs) regarding the

timing for the implementation of SP cooling. At the time of the inspection, the

inconsistency had not been resolved because Susquehanna did not recognize that it

impacted current plant operations. This performance deficiency has a cross-cutting

aspect in the area of Problem Identification and Resolution, Corrective Action Program,

because Susquehanna did not identify that the inconsistency documented in the CR

should have been categorized as a CAQ, commensurate with its safety significance.

P.1(a)

The performance deficiency is more than minor because it is associated with the Design

Control attribute of Mitigating Systems and affects the cornerstone objective to ensure

the availability, reliability, and capability of systems that respond to initiating events to

Enclosure

4

prevent undesirable consequences. Specifically, the EOPs provided direction that,

under some accident conditions, would affect the availability and/or capability of the SP

cooling system to perform its safety function. The finding screened out as having very

low safety significance because it was not a design deficiency, did not result in an actual

loss of safety function, and did not screen as potentially risk significant due to external

initiating events. (Section 4OA2.a.3 (b))

C Green: The NRC identified a Non-Cited Violation of 10 CFR 55.46(c)(1), Plant

Referenced Simulators, because the Susquehanna simulator did not accurately model

reactor pressure vessel (RPV) level instrumentation following a design basis accident

loss of coolant accident (DBA LOCA). Specifically, an analysis performed in 1994 to

determine if the observed simulator response during a large break LOCA was consistent

with the expected plant response, was based on an overly conservative assumption that

the drywell would experience superheated conditions, which would cause RPV water

level instrumentation reference leg flashing and a subsequent loss of all RPV level

indication. The expected plant response, as stated in the analysis, was incorrect; in that

a LOCA would not always cause a loss of all RPV level instruments. As a result, the

simulator modeling was incorrect.

The performance deficiency is more than minor because it is associated with the Human

Performance attribute of Mitigating Systems and affects the cornerstone objective to

ensure the availability, reliability, and capability of systems that respond to initiating

events to prevent undesirable consequences. Specifically, the modeling of the

Susquehanna simulator introduced negative operator training that could affect the ability

of the operators (a mitigating system) to take the appropriate actions during an actual

event. The finding was determined to be of very low safety significance because it is not

related to operator performance during requalification, it is related to simulator fidelity,

and it could have a negative impact on operator actions. (Section 4OA2.a.3 (c))

C Green: The NRC identified a Non-Cited Violation of 10 CFR 50, Appendix B, Criterion

XVI, Corrective Action, for the failure to identify that a setpoint error in the operating

procedures for safety-related systems was a condition adverse to quality (CAQ),

resulting in the procedures not being corrected in a timely manner. The setpoint for the

low pressure injection permissive interlock in the RHR and CS systems had been

changed in 1999 as part of a modification. However, the setpoint was not changed in

the system operating procedures and operator aids. When this issue was identified by

Susquehanna staff in 2006, the setpoint error in the procedure was not screened as a

CAQ, which resulted in the procedures not being revised for 17 months after the issue

was identified in an Action Report. This performance deficiency has a cross-cutting

aspect in the area of Problem Identification and Resolution, Corrective Action Program,

because Susquehanna did not identify that a setpoint error in operating procedures for

safety-related systems was a CAQ, commensurate with its safety significance. P.1(a)

The performance deficiency is more than minor because it is associated with the

Procedure Quality attribute of Mitigating Systems and affects the cornerstone objective

to ensure the availability, reliability, and capability of systems that respond to initiating

events to prevent undesirable consequences. Specifically, the incorrect setpoint

Enclosure

5

reference in the procedure impacted the reliability of operator response to the event in

that it could delay operator actions or result in misoperation of equipment. The finding

screened out as having very low safety significance because it was not a design

deficiency, did not result in an actual loss of safety function, and did not screen as

potentially risk significant due to external initiating events. (Section 4OA2.a.3 (e))

b. Licensee-Identified Violations

None.

Enclosure

6

REPORT DETAILS

4. OTHER ACTIVITIES (OA)

4OA2 Problem Identification and Resolution (PI&R) (Biennial - IP 71152B)

a. Assessment of the Corrective Action Program

1. Inspection Scope

The inspection team reviewed the procedures describing the corrective action program

(CAP) at the Susquehanna Steam Electric Station. Susquehanna used a single-point

entry system and identified problems by the initiation of an Action Request (AR). The

AR would then be sub-classified depending on the information provided; for example, as

WO for a maintenance Work Order, as CPG for assignment to the Central Procedure

Group, or as CR for a Condition Report. ARs were sub-classified as CRs for conditions

adverse to quality (CAQ), such as plant equipment deficiencies, industrial or radiological

safety concerns, or other significant issues. The CRs were subsequently screened for

operability and reportability, categorized by significance (1 to 3), assigned a level of

evaluation, and issued for resolution.

The team reviewed CRs selected across the seven cornerstones of safety in the NRC=s

Reactor Oversight Process (ROP) to determine if problems were being properly

identified, characterized, and entered into the CAP for evaluation and resolution. The

team selected items from the maintenance, operations, engineering, emergency

preparedness, physical security, radiation safety, training, and oversight programs to

ensure that Susquehanna was appropriately considering problems identified in each

functional area. The team used this information to select a risk-informed sample of CRs

that had been issued since the last NRC PI&R inspection, which was conducted in

February 2006.

The team selected ARs from other sub-classifications, to determine if Susquehanna had

appropriately classified these items as not needing to be a CR. The team also reviewed

operator log entries, control room deficiency lists, operator work-around lists, operability

determinations, engineering system health reports, completed surveillance tests, and

current temporary configuration change packages. In addition, the team interviewed

plant staff and management to determine their understanding of and involvement with

the CAP at Susquehanna. The CRs, and other documents reviewed, and the key

personnel contacted, are listed in the Attachment to this report.

The team considered risk insights from the NRC=s and Susquehanna=s risk analyses to

focus the sample selection and plant tours on risk-significant components. The team

determined that the five highest risk-significant systems at Susquehanna were

emergency service water, emergency diesel generators, residual heat removal service

water, station black-out diesel generator, and reactor core isolation cooling. For the

risk-significant systems, the team reviewed a sample of the applicable system health

Enclosure

7

reports, work requests and engineering documents, plant log entries, and results from

surveillance tests and maintenance tasks.

The team reviewed CRs to assess whether Susquehanna adequately evaluated and

prioritized the identified problems. The CRs reviewed encompassed the full range of

Susquehanna=s causal evaluations, including root cause analyses (RCA - to determine

the cause and prevent recurrence), apparent cause evaluations (ACE - to obtain a basic

understanding of the cause), and evaluations (to determine if a problem exists). The

review included the appropriateness of the assigned significance, the scope and depth

of the causal analysis, and the timeliness of the resolutions. For significant conditions

adverse to quality, the team reviewed the effectiveness of the corrective actions to

prevent recurrence. The team observed meetings of the CR Screening Team - in which

Susquehanna personnel reviewed new CRs for prioritization, and evaluated preliminary

corrective action assignments, analyses, and plans. The team also attended meetings

of the Corrective Action Review Board (CARB) - where senior managers reviewed

selected evaluations, effectiveness reviews, and extension requests.

The team reviewed equipment operability determinations, reportability assessments, and

extent-of-condition reviews for selected problems. The team assessed the backlog of

corrective actions in the maintenance, engineering, and operations departments, to

determine, individually and collectively, if there was an increased risk due to delays in

implementation of corrective actions. The team further reviewed equipment

performance results and assessments documented in completed surveillance

procedures, operator log entries, and trend data to determine whether the evaluations

were technically adequate to identify degrading or non-conforming equipment.

The team reviewed the corrective actions associated with selected CRs to determine if

the actions addressed the identified causes of the problems. The team reviewed CRs

for significant repetitive problems to determine if previous corrective actions were

effective. The team also reviewed Susquehanna=s timeliness in implementing corrective

actions. The team reviewed the CRs associated with selected non-cited violations

(NCVs) and findings to determine if Susquehanna properly evaluated and resolved these

issues.

2. Assessment

(a) Identification of Issues

In general, the team considered the identification of equipment deficiencies at

Susquehanna to be adequate. There was a low threshold for the identification of

individual issues, 23,000 ARs were written per year, and about 4,000 of those were

sub-classified as CRs. The housekeeping and cleanliness of the plant was generally

good; the general cleanliness of the plant enhanced the ability of personnel to more

easily identify equipment deficiencies and monitor equipment for worsening conditions.

Notwithstanding, during a tour of the facility, the inspectors observed that high density

concrete shield blocks were stacked on pallets in the vicinity of the Unit 1 recirculation

Enclosure

8

motor generator sets. The blocks were pre-staged for work during the upcoming

refueling outage, and were in a heavily trafficked area of the turbine building. There was

a painted warning on the floor, near the pallets, that the floor loading should not exceed

400 pounds per square foot (psf). When the inspectors asked whether the weight of the

blocks was within the rated floor load limit, it was determined that this condition had not

been identified and documented as acceptable. Initially, Susquehanna personnel

concluded that the blocks exceeded the posted limit and moved the pallets to reduce the

floor loading. Subsequently, Susquehanna weighed the pallets and blocks and

determined that they did not exceed the allowable floor loading. Based on this

evaluation the inspectors concluded the missed identification of this issue was minor.

The issue was documented in CR 954950.

The team also identified that several ARs were not classified as CRs, commensurate

with the safety significance, as required by their procedure (NDAP-QA-0702, Action

Request and Condition Report Process). The result was that the issues did not go to

the Screening Team, did not receive the necessary management attention, and were not

corrected in a timely manner (CR 957319). In addition, ARs are not normally trended to

allow the identification of an adverse change in performance. With the exception of the

first example, the below are considered procedure violations of minor significance due to

no impact on the related equipment. As such, these issues are not subject to

enforcement action, in accordance with the NRC=s Enforcement Policy.

Examples include:

C AR/CPG/OPS 751412, initiated February 2, 2006, identified that the Low Pressure

Injection Permissive setpoint was not changed in the residual heat removal (RHR)

and core spray (CS) operating procedures. The setpoint was changed in 1999, as

part of a modification; the procedures were not changed until July 2007. (See

Section 4OA2.a.3(d) for additional details.)

C AR/OPS/CSHIFT 777335, initiated July 25 2006, identified that an operator started

the suppression pool (SP) filter pump contrary to the procedure. The AR was closed

with no documented corrective actions taken.

The safety significance is that the operator did not operate the safety-related system

in accordance with the licensees written procedures and the Technical

Specifications (TS). The documentation of corrective actions should have included a

determination of the affects of starting of the pump, and counseling of the operator

on the requirement to follow procedures.

C AR/CPG 810513, initiated September 16, 2006, identified that the wrong valve

numbers were listed for the emergency service water (ESW) system valves for the

E EDG. As of the inspection, the procedure had not been changed.

The safety significance is that operators may not have been able to use the

licensees written procedure to align the ESW system in support of the operation of

the swing E EDG in a timely manner.

Enclosure

9

C AR/CPG/I&C 938054, initiated December 10, 2007, identified that a functional testing

and calibration procedure for the RHR service water radiation monitor could not be

performed, as written. As of the inspection, corrective actions had not been taken.

an inconsistency between the procedures and the design basis for SP cooling was a

CAQ, which resulted in corrective actions not being taken for two years to the time of the

inspection. Although the inconsistency was identified in 2006, Susquehanna personnel

did not recognize that the issue impacted current plant operations; as a result, the issue

was not scheduled for resolution in a timely manner. The team noted that, although

Susquehanna had classified the issue as a CR, it was considered to be NAQ - not a

CAQ - and was not scheduled for evaluation until the EPU had been approved. Refer to

Section 4OA2.a.3(b) for a detailed discussion of the finding.

(b) Prioritization and Evaluation of Issues

The team determined that Susquehannas performance in this area was adequate.

Notwithstanding the above discussion of some ARs not being classified as CRs, the

station appropriately reviewed those CRs that went to the Screening team and properly

classified them for significance. The discussions about specific topics at the Screening

meetings were detailed, and there were no classifications or immediate operability

determinations with which the team disagreed. The team considered the contributions of

the CARB to add value to the CAP process. One CARB review was noted to be

particularly insightful with respect to the quality of the causal analysis for CR 773046.

The CR identified problems with the closing of CRs by the nuclear training department

without completing all the required actions. The team did not identify any items in the

operations, engineering, or maintenance backlogs that were risk significant, individually

or collectively. In addition, the quality of the causal analyses reviewed was generally of

adequate technical detail and scope to identify causal factors and develop effective

corrective actions. The team noted that the RCA for the NCV from the last PI&R

inspection related to scaffolding was effective in that there had not been significant

recurrences of inadequate scaffold installations since the evaluation was completed.

With regard to operability evaluations, the team observed that, an operability

determination for the PAM level instruments, conducted in response to an inconsistency

between the FSAR and EOPs, determined that the level instruments would be operable.

(The inconsistency between the FSAR and the EOPs is described in detail in section

4OA2.a.3(b).) During follow-up discussions, the inspectors were told by operations and

engineering personnel that all of the PAM instrumentation together functioned to provide

the needed indications to the operators, and that the RPV level indications were not

needed after the initial entry into the EOPs. This was not consistent with the

requirements for the operability of each individual function of the PAM, as detailed in TS 3.3.3.1. Although subsequent discussions with the Susquehanna staff determined that

the most (if not all) of the PAM RPV level instruments would indicate post-LOCA, the

initial operability determination and statements during the inspection did not consider

that the PAM level instruments are required to be operable post-accident regardless of

whether EOPs have been entered. This issue was related to the performance

Enclosure

10

deficiencies discussed in findings 4OA2.a.3(a), (b) and (c), and is not identified as an

additional finding. The issue was entered into the CAP as AR/CR964836.

(c) Effectiveness of Corrective Actions

No findings of significance were identified in the area of effectiveness of corrective

actions. The team determined that the effectiveness of corrective actions at

Susquehanna was generally good. The control of scaffolds was a significant problem

during the last PI&R inspection; the team noted that oversight of scaffolds has improved,

but station personnel continue to identify examples where the scaffold does not appear

to be built in accordance with the procedure. In addition, the team identified

weaknesses in the scaffold procedure, such as allowing the installer to approve

deviations from the approved construction. During the inspection, the procedure was

revised, and plans were developed for engineering to review all current deviations.

3. Findings

(a) Failure to Adequately Evaluate a Deviation from BWROG EPG/SAG Resulted in an

Inadequate Procedure

Introduction: The NRC identified a Green NCV of 10 CFR 50, Appendix B, Criterion V,

Instructions, Procedures, and Drawings, because Susquehanna failed to adequately

evaluate a deviation from the Boiling Water Reactor Owners Group Emergency

Procedure Guidelines / Severe Accident Guidelines (BWROG EPG/SAG), which

resulted in one of the Emergency Operating Procedures (EOPs) being inadequate.

Description: On January 5, 2006, AR/CR 739371 was initiated to document an

inconsistency between the EOPs and assumptions in the Final Safety Analysis Report

(FSAR) regarding the initiation of suppression pool cooling. Specifically, it was identified

that the assumptions used in evaluating SP temperature response for the most limiting

design basis accident (DBA) loss of coolant accident (LOCA) did not appear to be

consistent with direction provided in the EOPs.

During this inspection, the team noted that the Susquehanna EOPs were not consistent

with the BWROG EPG/SAG. Specifically, BWROG EPG/SAG, Revision 2, Caution #1,

warned the operators that reactor pressure vessel (RPV) level instrumentation may be

unreliable if the temperatures near the instrument sensing lines exceeded RPV

saturation temperature. The EPG Bases stated that the purpose of Caution #1 was to

give the operators a chance to evaluate the validity of the RPV level instrumentation, in

order to avoid premature entry into the RPV flooding contingency procedure before it

was appropriate to do so. Susquehanna did not adequately evaluate the deviation from

the generic guidance in the EPG/SAG with respect to the caution. The Susquehanna

EOPs did not use a Caution statement, which would have allowed the operators the

opportunity to evaluate the level instrumentation; but instead, changed the caution to a

procedural step which directed the operators to transition directly to the RPV Flooding

procedure. Specifically, EO-100-103-1, Primary Containment Cooling, step DWT-3,

Enclosure

11

directed the operators to transition to contingency procedure EO-000-114-1, RPV

Flooding, when drywell temperature exceeded RPV saturation temperature.

The evaluation for the deviation was not completed in accordance with the requirements

of procedure NDAP-QA-0330, Symptom Oriented EOP and EP-DS Program and

Writers Guide. The procedure required that all deviations be evaluated to determine if

the deviation was technically justified and appropriate. Susquehanna documented that

the deviation was a minor difference from the generic guidelines in 50.59 Safety

Evaluation NL-92-019 (October 29, 1998) and 50.59 Screen 5059-01-976 (July 3, 2002).

The evaluation was based on an overly conservative assumption that all RPV level

instrumentation would be lost after a DBA LOCA. The reviews did not evaluate the

potential adverse consequences associated with the deviation, including the potential

impact on the SP cooling safety function. Immediate corrective actions included the

initiation of an informational Night Order to the control room operators explaining the

issue, and the cessation of all simulator scenarios that involve the use of EO-100-103-1

until the issue is resolved.

The performance deficiency is the failure to adequately evaluate a deviation from the

BWROG EPG/SAG, which resulted in one of the EOPs being inadequate for use by the

operators in the event of a DBA LOCA. Specifically, under some accident conditions,

the EOPs would have unnecessarily directed entry into RPV flooding which would have

limited the availability of SP cooling and complicated the operators response to the

event.

Analyses: This performance deficiency is more than minor because it is associated with

the Procedure Quality (EOP) attribute of the Mitigating Systems cornerstone and affects

the objective to ensure the availability, reliability, and capability of systems that respond

to initiating events to prevent undesirable consequences. Specifically, the EOP could

have directed entry into the RPV flooding procedure unnecessarily which would have

restricted the use of suppression pool cooling and required other actions that would have

complicated the operators response to the event. The inspectors performed a review of

the finding in accordance with NRC Inspection Manual Chapter (IMC) 0609,

Significance Determination Process (SDP), Attachment 4, Phase 1 - Initial Screening

and Characterization of Findings, and determined that the finding screened out as

having very low safety significance (Green), because it was not a design deficiency, did

not result in an actual loss of safety function, and did not screen as potentially risk

significant due to external initiating events.

Enforcement: 10 CFR 50, Appendix B, Criterion V, Instructions, Procedures, and

Drawings, states, in part, that activities affecting quality shall be prescribed by

documented procedures appropriate to the circumstances and that the activities shall be

accomplished in accordance with the procedures. Contrary to the above, Emergency

Operating Procedure EO-100-103-1, Primary Containment Cooling, was inadequate, in

that it directed the operators to transition directly to the RPV Flooding procedure when

RPV level instruments may have been available, which resulted in limiting the availability

of SP cooling. However, because the finding was of very low safety significance (Green)

Enclosure

12

and has been entered into the CAP (AR/CR 962881), this violation is being treated as an

NCV, consistent with section VI.A.1 of the NRC Enforcement Policy.

(NCV 05000387/2008006-01; 05000388/2008006-01 - Failure to Adequately Evaluate

a Deviation from BWROG EPG/SAG Resulted in an Inadequate EOP)

(b) Failure to Identify and Correct Inconsistencies Between the FSAR and the EOPs

Introduction: The NRC identified a Green NCV of 10 CFR 50, Appendix B, Criterion XVI,

Corrective Action, for the failure to identify that an inconsistency between the

emergency operating procedures and the design basis for SP cooling was a CAQ, which

resulted in corrective actions not being taken for two years to the time of the inspection.

Although the inconsistency was identified in 2006, Susquehanna personnel did not

recognize that the issue impacted current plant operations; as a result, the issue was not

scheduled for resolution in a timely manner. The assumption in the FSAR for the DBA

LOCA stated that SP cooling would be implemented ten minutes after entry into the

EOPs. The EOPs would not have allowed initiation of SP cooling for an extended period

of time.

Description: On January 5, 2006, AR/CR 739371 was initiated to document an

inconsistency between the EOPs and design basis assumptions for the SP cooling

response. The problem was identified during Susquehannas review in support of the

extended power uprate (EPU) project. Specifically, Susquehanna Engineering identified

that the assumptions used in evaluating SP temperature response for the most limiting

LOCA did not appear to be consistent with direction provided in the EOPs. The team

noted that, although Susquehanna personnel had classified the issue as a CR, they did

not recognize that the issue impacted current plant operations. Therefore, it was

considered to be NAQ - not a condition adverse to quality - and was not scheduled for

evaluation until the EPU had been approved.

The Susquehanna FSAR, Section 6.2.1.1.3, stated that the maximum SP temperature

would result from a reactor recirculation suction line break. The drywell pressure and

temperature response analyses assumed that RHR heat exchangers were activated

about ten minutes after entry into the EOPs to remove energy from the drywell by

cooling the SP. The CR identified that, in the event of a DBA LOCA, the EOPs would

direct operators to implement the RPV flooding procedure (EO-000-114) to maintain

adequate core cooling, and this required that all available RHR flow be used to flood the

RPV up to the steam lines. The initiators concern was that this would delay establishing

flow through a RHR heat exchanger for SP cooling, because of the unique design of the

RHR system at Susquehanna, and therefore would be inconsistent with the accident

analyses assumptions. In addition, the CR stated that it was assumed in the EOPs that

all RPV water level indications would be unreliable and therefore unavailable for this

scenario. Susquehanna personnel informed the team that they had not evaluated the

issues documented in the CR, at the time it was initiated, because they had assumed

that they were only associated with EPU and not current plant operation. Immediate

corrective actions included the start of an evaluation during the inspection of the

identified inconsistency for SP cooling, and additional guidance to the operators.

Enclosure

13

The performance deficiency is the failure to properly categorize the inconsistency

between the FSAR and the EOPs as a CAQ, which resulted in the deficiency not being

corrected in a timely manner commensurate with its safety significance.

Analyses: The performance deficiency is more than minor because it is associated with

the Design Control attribute of the Mitigating Systems cornerstone and affects the

objective to ensure the availability, reliability, and capability of systems that respond to

initiating events to prevent undesirable consequences. Specifically, in the event of a

DBA LOCA, SP cooling would not be initiated within the time frame assumed in the

FSAR, which could affect the capability of the system to perform its safety function

consistent with the design basis. The inspectors performed a review of the finding in

accordance with IMC 0609, and determined that the finding screened out as having very

low safety significance (Green) because it was not a design deficiency, did not result in

an actual loss of safety function, and did not screen as potentially risk significant due to

external initiating events.

This performance deficiency has a cross-cutting aspect in the area of Problem

Identification and Resolution (PI&R), Corrective Action Program (CAP), because

Susquehanna did not identify that the inconsistency documented in the CR should have

been categorized as a CAQ, commensurate with its safety significance. P.1(a)

Enforcement: 10 CFR 50, Appendix B, Criterion XVI, Corrective Action, states, in part,

that conditions adverse to quality shall be promptly identified and corrected. Contrary to

the above, Susquehanna failed to identify that the nonconformance identified in AR/CR

739371, January 2006, was a CAQ; this resulted in the condition not being corrected for

over two years. However, because the finding was of very low safety significance

(Green) and has been entered into the corrective action program (AR/CR 959670), this

violation is being treated as an NCV, consistent with section VI.A.1 of the NRC

Enforcement Policy.

(NCV 05000387/2008006-02; 05000388/2008006-02 - Failure to Identify and Correct

Inconsistencies Between the FSAR and the EOPs)

(c) Failure to Accurately Model the Simulator for RPV Water Level Instrumentation

Introduction: The NRC identified a Green NCV of 10 CFR 55.46(c)(1), Plant

Referenced Simulators, because the Susquehanna plant-referenced simulator did not

accurately model RPV level instrument response following a DBA LOCA. Specifically,

the RPV level instruments in the simulator were programmed to fail high after a LOCA,

and the expected plant response is that the instruments should indicate properly.

Description: As part of the teams follow-up on the issues in AR/CR 739371, the

inspectors questioned the concern stated in the CR, that the operators would need to

enter the RPV flooding procedure during a DBA LOCA due to a loss of valid RPV level

instrumentation. The inspectors reviewed the Susquehanna specific EOPs and

supporting documents, and determined that the Susquehanna EOP Plant Specific

Enclosure

14

Technical Guideline (PSTG) description of the expected response of the RPV level

instrument response to LOCA events, was based on analysis, EC-SIMU-1001,

Evaluation of Simulator Level Instrument Response to Large LOCA, dated May 4,

1994. The analysis was performed to determine if the observed simulator response

during a large break LOCA (RPV level instrumentation off-scale high) was consistent

with the expected plant response. The analysis assumed that the drywell would

experience superheated conditions, which would cause RPV water level instrumentation

reference leg flashing and a subsequent loss of all RPV level indication. The analysis

concluded that the simulator response reasonably predicted the expected actual plant

response during a large break LOCA event. The expected plant response, as stated in

the analysis, was incorrect; in that a LOCA would not always cause a loss of all RPV

level instruments.

On January 29, 2008, the inspectors observed two scenarios in the simulator to evaluate

the response to a DBA LOCA, with all safety systems available. The inspectors

observed that the RPV level instruments did indicate off-scale high shortly after the

initiation of the event, consistent with the analysis. The inspectors questioned the basis

of the analysis; specifically, why Susquehanna believed that the level instruments would

not be available after a DBA LOCA event. Subsequently, Susquehanna determined that

the RPV level instrument reference legs were not expected to routinely flash during a

DBA LOCA, and that the analysis had been based on an overly conservative assumption

that the drywell would always reach superheated conditions post-LOCA. Immediate

corrective actions included the initiation of an informational Night Order to the control

room operators explaining the issue, and the cessation of all simulator scenarios that

involve the use of EO-100-103-1 until the issue is resolved.

The performance deficiency is that Susquehanna did not ensure that the plant

referenced simulator accurately modeled the expected plant response for RPV level

instrumentation after a DBA LOCA, resulting in negative training of the licensed

operators.

Analyses: This performance deficiency is more than minor because it is associated with

the Human Performance attribute of the Mitigating Systems cornerstone and affects the

objective to ensure the availability, reliability, and capability of systems that respond to

initiating events to prevent undesirable consequences. Specifically, the incorrect

modeling of the Susquehanna plant referenced simulator introduces negative operator

training that could affect the ability of the operators (a mitigating system) to take the

appropriate actions during an actual event. The simulator training conditioned the

operators to expect the level instruments to be unavailable during events that cause

drywell temperatures to reach or exceed RPV saturation temperature. As a result,

during an actual event, the operators could prematurely transition into the RPV flooding

procedure when the RPV level instruments should be providing valid indication. The

inspectors evaluated the finding in accordance with IMC 0609, Appendix I, Licensed

Operator Requalification Significance Determination Process. The finding was

determined to be of very low safety significance (Green) because it is not related to

operator performance during requalification, it is related to simulator fidelity, and could

have a negative impact on operator actions.

Enclosure

15

Enforcement: 10 CFR 55.46(c)(1), Plant Referenced Simulators, states, in part, that a

plant referenced simulator must demonstrate expected plant response to normal,

transient, and accident conditions. Contrary to the above, as of January 2008, the

Susquehanna plant referenced simulator did not accurately demonstrate the actual

expected plant response of the RPV water level instrumentation following a DBA LOCA,

which could result in negative operator training. However, because the finding was of

very low safety significance (Green) and has been entered into the CAP (AR/CR

962881), this violation is being treated as an NCV, consistent with section VI.A.1 of the

NRC Enforcement Policy.

(NCV 05000387/2008006-03; 05000388/2008006-03 - Failure to Accurately Model

the Simulator for RPV Water Level Instrumentation)

(d) Failure to Identify and Correct a Setpoint Error in the RHR and CS Operating

Procedures

Introduction: The NRC identified a Green NCV of 10 CFR 50, Appendix B, Criterion XVI,

Corrective Action, for the failure to identify that a setpoint error in the operating

procedures for safety-related systems was a CAQ, resulting in the procedures not being

corrected in a timely manner. Specifically, in February 2006, Susquehanna personnel

identified an incorrect setpoint for the low pressure injection permissive interlock in the

RHR and CS systems operating procedures and associated hard cards; however, the

procedures were not revised until July 2007 due to the issue being screened as low

priority and not a condition adverse to quality (CAQ).

Description: On February 11, 2006, an AR was written to identify that the low pressure

injection permissive setpoint in the RHR and CS operating procedures, and the

associated operator hard cards, was incorrect. The correct setpoint is 420 pounds per

square inch gage (psig), but the procedures still had the previous setpoint of 436 psig.

The setpoint had been changed in 1999 as part of a modification. The procedures were

not revised until July 16, 2007, 17 months after the deficiency was identified in an AR. In

addition, the inspectors noted that the setpoint in the procedures (436 psig) was not

within the allowable tolerance (407-433 psig) listed in the Susquehanna TS, Section 3.3.5.1, Emergency Core Cooling System (ECCS) Instrumentation.

When the AR was initiated, it was sub-classified as AR/CPG/OPS; that is, assigned to

the Central Procedures Group and identified as an Operations procedure. It was not

recognized that deficient operating procedures for safety-related systems may be a CAQ

and that the AR should have been classified as a Condition Report. The affected

section in the procedures was the verification of the response of the systems to an

automatic initiation signal. For example, the Unit 1 RHR procedure OP-149-001, RHR

System, Section 2.2, noted that No operator action is required unless an automatic

action failed to occur ... At 436 psig decreasing Reactor pressure, RHR INJ OB ISO

[injection outboard isolation] HV-151-F015A & B OPEN. If the valves did not open at

the specified pressure in the procedure and hard card, the operator may have diverted

their attention unnecessarily and attempted to open the valve manually, even though the

Enclosure

16

interlock would not have been satisfied (420 psig) and the valve would not open in

accordance with the plant design.

The pressure switches were changed in 1999, as part of a Unit 1 plant modification

(Design Change Package (DCP) 97-9075); Unit 2 switches were changed by DCP

97-9076. The modification replaced the existing pressure switches with Barton pressure

indicating switches, because of improved accuracy. The low pressure injection

permissive interlock prevents the CS and RHR injection valves from opening until

reactor pressure has decreased to the RHR and CS systems design pressure, to

prevent over pressurization of the RHR and CS systems. The DCP identified the

specific RHR and CS operating procedures as needing to be changed. Immediate

corrective actions included the initiation of a new CR to evaluate the other pending

procedure changes to determine if their priority should be revised.

The performance deficiency involved a failure to identify and correct a CAQ, the

incorrect setpoint, in a timely manner commensurate with its safety significance. The

inspectors concluded this action was untimely because the modification process would

have revised these procedures prior to the modification being accepted by operations

personnel.

Analysis: The performance deficiency is more than minor because it is associated with

the Procedure Quality attribute of the Mitigating Systems cornerstone and affects the

objective to ensure the availability, reliability, and capability of systems that respond to

initiating events to prevent undesirable consequences. Specifically, the incorrect

setpoint reference in the procedure impacted the reliability of operator response to the

event in that it could delay operator actions or result in misoperation of equipment. The

inspectors performed a review of the finding in accordance with NRC Inspection Manual

Chapter (IMC) 0609, Significance Determination Process (SDP), Attachment 4, Phase

1 - Initial Screening and Characterization of Findings. The inspectors determined that

the finding screened out as having very low safety significance (Green), because it was

not a design deficiency, did not result in an actual loss of safety function, and did not

screen as potentially risk significant due to external initiating events

This performance deficiency has a Cross-Cutting aspect in the area of PI&R, CAP,

because Susquehanna did not identify that a setpoint error in operating procedures for

safety-related systems was a CAQ, commensurate with its safety significance. P.1(a)

Enforcement: 10 CFR 50, Appendix B, Criterion XVI, Corrective Action, states, in part,

that conditions adverse to quality shall be promptly identified and corrected. Contrary to

the above, from 1999, when the pressure switches were replaced and the setpoint was

changed, until 2006, when AR 751412751412was written, Susquehanna had failed to identify

that the setpoint was wrong for the low pressure injection permissive interlock in the

operating procedures for RHR and CS. Subsequently, on February 11, 2006, when

Susquehanna personnel initiated and approved AR 751412751412 they failed to identify that

the stated deficiency was a CAQ, which resulted in untimely corrective actions.

Susquehanna considered this to be a procedure change and not a CAQ, and classified

the AR as a CPG versus a CR. As such, the procedures were not changed until July 16,

Enclosure

17

2007, 17 months after the condition was identified and eight years after the setpoint was

changed in the plant. Because this finding is of very low safety significance (Green), and

was entered into the Susquehanna CAP (AR/CR 956917) this violation is being treated

as a Non-Cited Violation (NCV) consistent with Section VI.A.1 of the NRC Enforcement

Policy.

(NCV 05000387/2008006-04; 05000388/2008006-04 - Failure to Identify and Correct

a Setpoint Error in the RHR and CS Operating Procedures)

b. Assessment of the Use of Operating Experience

1. Inspection Scope

The team reviewed a sample of operating experience (OE) issues for applicability to

Susquehanna, and for the associated actions. The documents were reviewed to ensure

that underlying problems associated with the issues were appropriately considered for

resolution. The team also reviewed how Susquehanna considered OE for applicability in

causal evaluations.

Prior to the start of the inspection, the inspectors noted a potential negative trend in the

number of issues associated with reactivity management. In accordance with the

Inspection Procedure, the inspectors increased the scope of the review to determine if

there was an adverse trend in the area of reactivity management over the past five

years. The inspectors reviewed select ARs and CRs associated with the control rod

drive system, control rod problems, human performance issues, and the spent fuel pool;

the inspectors review included how Susquehanna had incorporated applicable OE for

these specific systems and human performance issues into the CAP. The inspectors

interviewed selected licensee staff.

2. Assessment

In general, OE was effectively used at the station. The inspectors noted that OE was

reviewed during the causal evaluation process and incorporated, as appropriate, into the

development of the associated corrective actions. The inspectors noted that OE was

frequently used in work packages and pre-job briefs. The team did not identify any

significant deficiencies within the sample reviewed. The team did not identify a negative

trend nor any significant problems with the control of activities associated with reactivity

management.

3. Findings

No findings of significance were identified in the area of operating experience.

c. Assessment of Self-Assessments and Audits

1. Inspection Scope

Enclosure

18

The team reviewed a sample of departmental self-assessments, CAP trend reports, and

Quality Assurance (QA) audits, including QAs most recent audit of the CAP. The team

also reviewed the latest internal assessment of the safety culture at Susquehanna,

conducted in October 2006. The reviews were performed to determine if problems

identified through these evaluations were entered into the CAP system, and whether the

corrective actions were properly completed to resolve the deficiencies. The

effectiveness of the audits and self-assessments was evaluated by comparing audit and

self-assessment results against self-revealing and NRC-identified findings, and

observations during the inspection.

2. Assessment

The team considered the quality of the audits and self-assessments to be thorough and

critical. ARs were initiated for issues identified by QA and the self-assessments. The

Susquehanna 2006 Comprehensive Cultural Assessment Report consisted of a safety

culture survey and interviews. The cultural assessment report identified some

weaknesses at the station, which were entered into the CAP. The team did not identify

any results that were inconsistent with Susquehannas conclusions.

3. Findings

No findings of significance were identified in the area of audits and self-assessments.

d. Assessment of Safety Conscious Work Environment

1. Inspection Scope

To evaluate the safety conscious work environment (SCWE) at Susquehanna, during

interviews and discussions with station personnel, the team assessed the workers

willingness to enter issues into the CAP and to raise safety issues to their management

and/or to the NRC. The inspectors also interviewed the Employee Concerns Program

(ECP) representative to determine if employees were aware of the program and had

used it to raise concerns. The team reviewed a sample of the ECP files to ensure that

issues were entered into the corrective action program, as appropriate.

2. Assessment

Based on interviews, observations of plant activities, and reviews of the ARs and ECP,

the inspectors determined that the site personnel were willing to raise safety issues and

document them in ARs. Individuals actively utilized the AR system, as evidenced by the

number and significance of issues entered into the program. The inspectors noted that

ARs were written by a variety of personnel, from workers to managers. ECP evaluations

were thorough and appropriate actions were taken to address issues.

3. Findings

No findings of significance were identified related to the SCWE at Susquehanna.

Enclosure

19

4OA6 Meetings, Including Exit:

On February 1, 2008, the team presented the inspection results to Mr. B. McKinney,

Senior Vice President, and to other members of the Susquehanna staff, who

acknowledged the findings. The team confirmed that no proprietary information

reviewed during the inspection was retained.

ATTACHMENT: Supplemental Information

In addition to the documentation that the team reviewed (listed in the Attachment),

copies of information requests given to the licensee are in ADAMS, under accession

number ML080430585.

Enclosure

A-1

ATTACHMENT - SUPPLEMENTAL INFORMATION

KEY POINTS OF CONTACT

Licensee Personnel:

M. Adelizzi, Risk Engineer

N. DAngelo, Manager, Station Engineering

C. Gannon, Vice President, Nuclear Operations

T. Gorman, Project Manager, Design Engineering

R. Hoffman, Manager, Nuclear Fuels & Analysis

B. McKinney, Chief Nuclear Officer

I. Missien, Project Manager, System Engineering

B. ORourke, Senior Engineer, Nuclear Regulatory Affairs

R. Pagodin, General Manager, Nuclear Engineering

R. Paley, General Manager, Plant Support

A. Price, Supervisor, Corrective Action & Assessment

M. Rochester, Employee Concerns Representative

G. Ruppert, Manager, Maintenance

R. Schechterly, Operating Experience Coordinator

R. Sgarro, Manager, Nuclear Regulatory Affairs

M. Sleigh, Security Manager

B. Stitt, Operations Training

T. Tonkinson, Supervisor, Maintenance Support

D. Weller, Maintenance Foreman

L. West, Supervisor, Central Procedure Group

Nuclear Regulatory Commission:

M. Gray, Branch Chief, Technical Support & Assessment

F. Jaxheimer, Senior Resident Inspector

LIST OF ITEMS OPENED, CLOSED, AND DISCUSSED

Opened and Closed:

05000387/2008006-01 NCV Failure to Adequately Evaluate a Deviation from BWROG EPG/SAG

05000388/2008006-01 Resulted in an Inadequate EOP (Section 4OA2.a.3 (a))05000387/2008006-02 NCV Failure to Identify and Correct Inconsistencies in the Licensing Basis05000388/2008006-02 and the EOPs (Section 4OA2.a.3 (b))05000387/2008006-03 NCV Failure to Accurately Model the Simulator for RPV Water Level

05000388/2008006-03 Instrumentation (Section 4OA2.a.3 (c))05000387/2008006-04 NCV Failure to Identify and Correct a Setpoint Error in the RHR and CS

05000388/2008006-04 Operating Procedures (Section 4OA2.a.3 (d))

Attachment

A-2

LIST OF DOCUMENTS REVIEWED

Procedures:

BWROG EGP/SAG and Appendix B Bases, Revision 2

Design Considerations Applicability Sheet Number 42, Emergency Plan, Revision 1

EO-000-102, RPV Control, Revision 2

EO-000-114-1, RPV Flooding, Revision 5

EO-100-103-1, Primary Containment Control, Revision 9

EP-AD-014, Surveillance Testing of Emergency Communications Equipment, Revision 10

EP-AD-015, Review, Revision, and distribution of the SSES Emergency Plan, Revision 11

ME-0RF-161, Control of Fuel Pool Cleanout Activities, Revision 5

ME-0RF-163, Fuel Pool Cleanout - Energy Solutions - Dose Rate Profiling of Irradiated

Hardware and Liners, Revision 4

MFP-QA-1220, Engineering Change Process Handbook, Revision 2

MI-VL-009, Operation of Leak Rate Monitors, Surge Tank Assemblies and 1035 psig Test

Pumps, Revision 3

MT-AD-504, Scaffold Erection, Review and Inspection, Revisions 9 & 10

MT-GM-018, Freeze Sealing of Piping, Revision 15

MT-GM-050, Limitorque Type SMB-000 through SMB-4 Operator Maintenance, Revision 12

NASP-QA-202, Independent Technical Review Program, Revision 2

NASP-QA-401, Internal Audits, Revision 9

NASP-QA-700, Performance Assessment Process, Revision 0

NDAP-00-0109, Employee Concerns Program, Revision 10

NDAP-00-0708, Corrective Action Review Board, Revision 4

NDAP-00-0710, Station Trending Program, Revision 1

NDAP-00-0745, Self-Assessment, Benchmarking and Performance Indicators, Revision 7

NDAP-00-0751, Significant Operating Experience Report (SOER) Review Program, Revision 3

NDAP-00-0752, Cause Analysis, Revisions 3 and 4

NDAP-00-0753, Common Issue Analysis, Revision 0

NDAP-00-0778, Performance Improvement Program, Revision 2

NDAP-QA-0103, Audit Program, Revision 9

NDAP-QA-0330, PSTG and Emergency Procedures, Revision 8

NDAP-QA-0330, Symptom Oriented EOP and EP-DS Program and Writers Guide, Revision 3

NDAP-QA-0412, Leakage Rate Test Program, Revision 10

NDAP-QA-0702, Action Request and Condition Report Process, Revision 20

NDAP-QA-0703, Operability Assessments and Requests for Enforcement Discretion,

Revision 12

NDAP-QA-0720, Station Report Matrix and Reportability Evaluation Guidance, Revision 13

NDAP-QA-0725, Operating Experience Review Program, Revision 11

NDAP-QA-0726, 10CFR50.59 and 10CFR72.48 Implementation, Revision 10

NDAP-QA-1220, Engineering Change Process, Revision 2

NTP-QA-53.1, Susquehanna Fire Brigade Training Program, Revision 15

ODCM-QA-001, ODCM Introduction, Revision 3

ODCM-QA-002, ODCM Review and Revision Control, Revision 4

ODCM-QA-003, Effluent Monitor Setpoints, Revision 3

ODCM-QA-004, Airborne Effluent Dose Calculations, Revision 4

ODCM-QA-005, Waterborne Effluent Dose Calculation, Revision 3

Attachment

A-3

ODCM-QA-006, Total Dose Calculation, Revision 2

ODCM-QA-007, Radioactive Waste Treatment Systems, Revision 2

ODCM-QA-008, Radiological Environmental Monitoring Program, Revision 11

ODCM-QA-009, Dose Assessment Policy Statements, Revision 2

ON-145-004, RPV Water Level Anomaly, Revision 13

OP-024-001, Diesel Generators, Revision 49

OP-024-004, Transfer and Test Mode Operations of Diesel Generator E, Revision 26

OP-149-001, RHR System, Revisions 31 and 32

OP-151-001, Core Spray System, Revisions 27 & 28

SE-124-007, Unit 1 Division 1 Diesel Generator LOCA LOOP Test, Revision 15

SE-259-044, LLRT of RHR Containment Spray Penetration Number X-39A, Revision 11

SOP-054-B03, Quarterly ESW Flow Verification Loop B, Revision 7

SSES-EPG, SSES Plant Specific Technical Guideline, Revision 9

Audits:

666178, Corrective Action, November 2006 - February 2007

667966, QA Internal Audit Report, Fuel Management, Revision 0

691277, QA Internal Audit Report Access Authorization and Fitness for Duty, Revision 0

706249, Operations Training and Qualification Programs, May - June 2007

718607, QA Internal Audit Report, Engineering, Revision 0

744333, Operations, November - December 2007

792034, QA Internal Audit Report, Security, Revision 0

NEIP Audit of Susquehanna Quality Assurance, June 2006

Self-Assessments:

2006 Comprehensive Cultural Assessment, September - October 2006

CA&A Functional Unit Excellence Plan, 1st, 2nd, and 3rd Quarters 2007

CAA-06-01, Site Wide Self-Assessment, December 2006

CAA-06-05, Self-Assessment Program Performance, February 2006

CAA-06-08, Decrease in CR Generation Identified by Trend Report, November 2006

Focused Self Assessment, MOV Program Self-Assessment, October 2007

Maintenance Implementing Procedures Adequacy for Qualified, Inexperienced Employees,

June 2007

Multi-Utility Joint Audit Program Initiative, March - April 2007

NTG Focused Self-Assessment of Operator Training Programs, June 2007

OPS-06-02, Determine the Status of Operator Fundamentals, February 2006

OPS-06-03, Operations Focused Se-f Assessment, July 2006

Pre-PI&R Focused Self-Assessment, September 2007

QA Organization Effectiveness Self-Assessment, October 2006

QA-06-01, Operations QA Audit Preparation Gap Analysis for QC, May - July 2006

SEC-06-01, Analyses of SSES Security Procedures and Physical Security Plan, Revision 0

Attachment

A-4

Action Requests (* denotes an AR/CR generated as a result of this inspection):

478369 724467 741707 759209 779830 810391 843985 873741 896685 941677

524893 724717 741908 759216 780144 810513 845441 873919 897250 941810

542157 726672 741943 759827 780155 811239 849935 874227 898909 947160

545804 728295 742191 760281 780778 811429 851918 875597 899429 954950*

549328 728936 742318 760526 780992 811996 853358 875976 900301 954970*

554362 730852 742342 760526 781644 812948 854681 876021 900720 954972*

554598 730944 742427 762497 782321 813844 855266 876427 901262 954975*

555140 730947 742676 763050 782344 815268 855268 877419 903439 954990*

555263 737236 742966 763128 783655 816097 856997 877727 904689 955072*

555562 738555 743043 763397 784730 816710 858269 877743 908163 955073*

557348 738575 744975 764145 784882 817720 858578 878165 911601 955111*

565795 738634 744979 764738 784890 818082 859082 878326 912213 955130*

575128 738653 745221 764953 785561 818154 859440 879080 912476 955150*

578943 738907 745248 765421 785791 820344 859794 879847 915167 955151*

584400 738999 745462 767566 786149 820380 859839 880331 915620 955761*

591033 739262 745773 767567 786224 820989 860299 880573 916453 955780*

594366 739371 746658 768301 786564 820995 860551 880702 916463 956339*

594887 739371 747077 768502 786735 821006 861162 880806 916873 956344*

595165 739386 747438 768821 786768 821064 861366 881210 917196 956431*

604009 739419 749294 768920 787850 822996 861415 881219 918392 956696*

604296 739579 749341 769304 788616 823908 862474 881225 918549 956914*

610978 739625 749832 769867 788621 824522 864090 881236 919470 956917*

615707 739713 750140 769870 788879 824895 865286 882318 927046 957319*

623914 739737 750232 770453 789971 825107 865423 883987 928515 957484*

623949 740043 751212 771319 791115 825750 865804 886209 929461 957637*

635924 740073 751412 771876 791329 826452 865924 887048 930075 958769*

647827 740303 751433 771961 792158 826870 866930 887067 930571 959670*

655735 740477 751444 773046 793381 827023 867534 888310 931113 961655

666405 740538 752341 773409 794995 827966 867747 889683 932590 962390

668871 740658 752347 774453 795583 828626 867881 889966 936060 962881*

669732 740668 752582 774475 796640 828744 868251 891288 936250 963061*

677145 740723 753392 774509 797517 829065 868259 891733 936370 963065*

687080 740802 753664 774549 799890 829502 868828 891795 936631 963698*

688300 740804 753869 775285 802254 835002 868874 892142 937123 963861*

691108 740825 753990 775718 802539 837153 869819 892152 938054 964512*

693936 740946 755360 776112 802563 837180 869824 892528 938698 964514*

699781 740948 756094 776171 802572 839753 870968 893090 938722 964836*

723483 740955 756415 776769 802697 841169 871013 893157 939516 965167*

723976 740988 756804 776918 805698 841885 872039 893290 939780

724102 741041 757530 777335 806710 842663 872056 895147 941290

724165 741321 757979 777723 809503 842920 873026 896455 941401

724374 741457 758337 778124 809702 843144 873683 896505 941626

Attachment

A-5

Maintenance Work Requests (SPWO):

099065 099364 766396 766413 767284 768234 862569

099115 448229 766401 766416 767490 768618 862578

099120 473889 766406 766496 767506 818282 866262

099259 570758 766411 767283 767532 862503 866284

Non-Cited Violations and Findings Reviewed:

NCV 2005005-01, Inadequate FME Exclusion Procedural Instructions Associated with EDG

Work

FIN 2005009-01, Fire Brigade Drill Program Not Consistent with Regulatory Guidance and

Industry Standards

NCV 2006002-01, Equipment Hatch Plugs are Not Watertight as Indicated in FSAR

FIN 2006002-02, Incomplete Corrective Actions Contribute to CRD Flow Control Failure

NCV 2006003-01, Inadequate Procedures Resulted in Motor Operated Valve Failures

NCV 2006003-02, Failure to Identify Material Degradation which Resulted in the Failure of the

C ESW Pump Breaker

NCV 2006003-03, Inadequate Procedure Results in Elevated Reactor Coolant System Leakage

NCV 2006003-04, Inadequate Design Review of PRDNMS Modification Resulted in a Reactor

Scram

NCV 2006003-05, Ineffective Corrective Actions to Assure Training and Qualification of Workers

as Required by 10CFR50, Appendix B, Criterion XVI

NCV 2006004-01, Inadequate Risk Assessment

NCV 2006005-01, Inadequate Work Instructions for the Disassembly and Inspection of Check

Valves

NCV 2006005-02, Inadequate Evaluation of EPA Breaker Failures

NCV 2006006-01, Failure to Identify Scaffolding that Affected the Safety-Related RHR

Discharge Pressure Instrument Tubing Input to ADS

NCV 2006009-01, Safeguards Information

Licensee Identified NCV 2007002, U2 Div II Core Spray Pump Room (a High Radiation Area)

Was Not Posted and Was Open

Licensee Identified NCV 2007002, U1 HPCI Failed a Surveillance Due to the Failure to Perform

Preventive Maintenance

NCV 2007003-01, Failure to Take Timely Corrective Actions for an E EDG Jacket Water Leak

FIN 2007003-02, Failure to Maintain Occupational Radiation Exposure ALARA during Reactor

Water Cleanup Pipe Replacement Activities

FIN 2007003-03, Failure to Maintain Occupational Radiation Exposure ALARA during Outage

ISI of Reactor Pressure Vessel

NCV 2007003-04, Violation of 10CFR71.5 for Inadequately Secured Transport of Condensate

Pump Motors

NCV 2007003-05, Violation of 10CFR71.5 for Inadequately Accounting for Activity in a

Shipment of Irradiated Fuel Channels

Licensee Identified NCV 2007003, U2 Reactor Building HRA Postings and Boundary Moved

without Permission of RP

NCV 2007007-01, Inoperable ESSW Pump-House Ventilation Lineup

NCV 2007007-02, Failure to Use E EDG Procedure

Attachment

A-6

Miscellaneous:

5059-01-2356, 50.59 Screen of Specification C-1056, Long Term Scaffolding, Revision 4

CP067, Corrective Action Program - Evaluation & Resolution, Revision 8

(Lesson Plan & Student Material)

CP068, Managing the Corrective Action Process, Revision 2 (Lesson Plan & Student Material)

Daily CR Screening Team Package

Design Verification Checklist for SCN 6 for Specification C-1056, dated April 27, 2001

EC-059-1024, Design Requirements for and Evaluation of Potential Secondary Containment

Bypass Leakage Pathways, Revision 4

EC-RADN-1029, SSES Design Basis LOCA Dose Consequence Evaluation for Containment

Bypass Leakage Including the Effects of Suppression Pool Scrubbing, Revision 1

EC-SIMU-1001, Evaluation of Simulator Level Instrument Response to Large LOCA, dated

May 4, 1994

Engineering Specification C-1056, Erection of Scaffolding in Safety-Related Areas, Revision 4

EWR #MIS-85-0460, Design Inputs and Considerations Checklist for Specification C-1056,

Revision 2

Hot Box Item 08-01, Reactor Water Instrumentation Response during DBA LOCA, dated

January 31, 2008

IEEE Standard 497-2002, IEEE Standard Criteria for Accident Monitoring Instrumentation, dated

September 30, 2002

Long Term Scaffold Log, dated January 16, 2008

No Degraded Condition Response to OFR 963310, dated January 30, 2008

NRC Information Notice 2007-29, Temporary Scaffolding Affects Operability of Safety-Related

Equipment, dated September 17, 2007

NRC Inspection Procedure 42001, Emergency Operating Procedures, dated June 28, 1991

NRC Regulatory Guide 1.97, Instrumentation for Light-Water-Cooled Nuclear Power Plants to

Assess Plant and Environs Conditions During and Following an Accident, Revision 2

NRC Regulatory Issue Summary 2005-20, Information to Licensees Regarding Two NRC

Inspection Manual Sections on Resolution of Degraded and Nonconforming Conditions and

on Operability

NRC Regulatory Issue Summary 2007-21, Adherence to Licensed Power Limits, dated

August 23, 2007

NEDE-24801, Review of BWR Reactor Vessel Water Level Measurement, April 1980

NEDO-24708A, Additional Information Required for NRC Staff Generic Report on Boiling Water

Reactors, Revision 1

Operational Policy Statement (OPS) - 5, Deficiency Control System, Revision 13

Operations Monthly Performance Indicators, December 2007

Operations Quality Assurance Manual, dated December 13, 2007

OPEX Daily Report, January 29, 2008

Plant Modification Package - DCP/ECO #97-9075, Unit 1 Core Spray/RHR/LPCI Pressure

Switch Replacement, Revision 1

PL-NF-02-07, Channel Management Action Plan, Revision 28

Regulatory Guide 1.97, Criteria for Accident Monitoring Instrumentation, Revision 4

Specification Change Notice #6 for C-1056, Revision 3

Temporary Scaffold Log, dated January 15, 2008

Unit 1 & 2, Control Rod Drive Hydraulics System Health Report, May - August 2007

Unit 1, RHR Residual Heat Removal System Health Report, September - December 2007

Attachment

A-7

LIST OF ACRONYMS

ACE Apparent Cause Evaluation

AR Action Request

BWROG Boiling Water Reactor Owners Group

CAP Corrective Action Program

CAQ Condition Adverse to Quality

CARB Corrective Action Review Board

CFR Code of Federal Regulations

CPG Central Procedure Group

CR Condition Report

CS Core Spray

DBA Design Basis Accident

DCP Design Change Package

ECCS Emergency Core Cooling System

ECP Employee Concerns Program

EOP Emergency Operating Procedures

EPG/SAG Emergency Procedure Guidelines / Severe Accident Guidelines

EPU Extended Power Uprate

FSAR Final Safety Analysis Report

IMC NRC Inspection Manual Chapter

LOCA Loss of Coolant Accident

NCV Non-Cited Violation

NRC Nuclear Regulatory Commission

OE Operating Experience

PAM Post-Accident Monitoring

PI&R Problem Identification and Resolution

psig pounds per square inch

PSTG Plant Specific Technical Guidelines

QA Quality Assurance

RCA Root Cause Analysis

RHR Residual Heat Removal

ROP Reactor Oversight Program

RPV Reactor Pressure Vessel

SCWE Safety Conscious Work Environment

SDP Significance Determination Process

TS Technical Specifications

Attachment