ML17223B066: Difference between revisions
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{{#Wiki_filter:t 6 ACCELERATED DIjRIBUTION DEMONSTiTION SYSTEM REGULATORY INFORMATION DISTRIBUTION SYSTEM (RIDS)ESSION NBR: 9101280251 DOC.DATE: 91/01/26 NOTARIZED: | {{#Wiki_filter:t 6 ACCELERATED DIjRIBUTION DEMONSTiTION SYSTEM REGULATORY INFORMATION DISTRIBUTION SYSTEM (RIDS) | ||
NO FACIL:50-335 St.Lucie Plant., Unit 1, Florida Power&Light Co.50-389 St.Lucie Plant, Unit 2, Florida Power&Light Co.AUTH.NAME AUTHOR AFFILIATION GOLDBERG,J.'H. | ESSION NBR: 9101280251 DOC. DATE: 91/01/26 NOTARIZED: NO DOCKET FACIL:50-335 St. Lucie Plant., Unit 1, Florida Power & Light Co. 05000335 50-389 St. Lucie Plant, Unit 2, Florida Power & Light Co. 05000389 AUTH. NAME AUTHOR AFFILIATION GOLDBERG,J.'H. Florida Power & Light Co. | ||
Florida Power&Light Co.RECIP.NAME RECIPIENT AFFILIATION Document Control Branch (Document Control Desk)SUM'ECT: Clarifies 900413 response to violations noted in Insp Repts 50-335/90-02 | RECIP.NAME RECIPIENT AFFILIATION Document Control Branch (Document Control Desk) | ||
&50-389/90-02.Corrective actions:nuclear job planning sys changed to include speed governor oil changes consistent w/vendor recommendations. | SUM'ECT: Clarifies 900413 response to violations noted in Insp Repts 50-335/90-02 & 50-389/90-02.Corrective actions:nuclear job planning sys changed to include speed governor oil changes consistent w/vendor recommendations. | ||
DISTRIBUTION CODE: ZE01D COPIES RECEIVED:LTR | DISTRIBUTION CODE: ZE01D COPIES RECEIVED:LTR ENCL SIZE: | ||
~J.H. | TITLE: General (50 Dkt)-Insp Rept/Notice of Vio ation Response NOTES: | ||
PLEASE HELP US TO REDUCE WASTE!CONTACT THE DOCUMENT CONTROL DESK, ROOM P 1-37 (EXT.20079)TO | RECIPIENT COPIES RECIPIENT COPIES ID CODE/NAME LTTR ENCL ID CODE/NAME LTTR ENCL PD2-2 PD NORRIS,J INTERNAL: ACRS 2 AEOD 1 AEOD/DEIIB 1 AEOD/TPAB 1 DEDRO 1 NRR MORISSEAU,D 1 NRR SHANKMAN,S 1 NRR/DLPQ/LPEB10 1 NRR/DOEA/OEAB 1 NRR/DREP/PEPB9 D 1 NRR/DRIS/DIR 1 - NRR/DST/DIR 8E2 1 NRR/PMAS/ILRB12 1 NUDOCS-ABSTRACT 1 OE DI 1 OGC/HDS2 ib RE ~FILE 0 1 RGN2 FILE 01 1 EXTERNAL: EG&G/BRYCE ~ J. H. NRC PDR NSZC NOTE TO ALL "RIDS" RECIPIENTS: | ||
PLEASE HELP US TO REDUCE WASTE! CONTACT THE DOCUMENT CONTROL DESK, ROOM P 1-37 (EXT. 20079) TO ELliVIINATEYOUR NAME FROM DISTRIBUTION LISTS FOR DOCUMENTS YOU DON'T NEED! | |||
TOTAL NUMBER OF COPIES REQUIRED: LTTR 24 ENCL Q | |||
P.O.Box14000, Juno Beach, FL 33408-0420 JANUARY 2 4 1991 L-91-26 U.S.Nuclear Regulatory Commission Attn: Document Control Desk Washington, D.C.20555 Gentlemen: | P.O. Box14000, Juno Beach, FL 33408-0420 JANUARY 2 4 1991 L-91-26 U. S. Nuclear Regulatory Commission Attn: Document Control Desk Washington, D. C. 20555 Gentlemen: | ||
Re: St.Lucie Unit 1 and 2 Docket Nos.50-335 and 50-389 Response to Notice of Violation Clarification Ins ection Re ort 90-02 Reference A: St.Lucie Unit 1 and 2 Docket Nos.50-335 and 50-389 Response to Notice of Violation Ins ection Re ort 90-02 L-90-138, dated April 13, 1990 On January 10, 1991, a discussion between NRC Region II personnel and the St.Lucie Plant staff resulted in a request by the | Re: St. Lucie Unit 1 and 2 Docket Nos. 50-335 and 50-389 Response to Notice of Violation Clarification Ins ection Re ort 90-02 Reference A: St. Lucie Unit 1 and 2 Docket Nos. 50-335 and 50-389 Response to Notice of Violation Ins ection Re ort 90-02 L-90-138, dated April 13, 1990 On January 10, 1991, a discussion between NRC Region II personnel NRC for and the St. Lucie Plant staff resulted in a request by the clarification of the "specific procedures" mentioned in Finding B, Response 3, in Reference A. In Reference A, Florida Power & Light Company (FPL) stated: | ||
: 3. The specific vendor recommendation regarding the speed governor oil change was completed. The specific procedures | |||
- | |||
were changed to reflect the oil changes at a frequency consistent with the vendor's recommendation. | |||
FPL submits the following clarification: | FPL submits the following clarification: | ||
The Nuclear Job Planning System (NJPS)was changed to include the speed governor oil changes at a frequency consistent with the vendor's recommendation on February 2, 1990.The NJPS is a system designed to ensure preventative maintenance is scheduled within the desired time frames and tracked to completion. | The Nuclear Job Planning System (NJPS) was changed to include the speed governor oil changes at a frequency consistent with the vendor's recommendation on February 2, 1990. The NJPS is a system designed to ensure preventative maintenance is scheduled within the desired time frames and tracked to completion. | ||
A detailed set of written work instructions was developed using the guidance in the vendor technical manual to perform the required preventative maintenance. | A detailed set of written work instructions was developed using the guidance in the vendor technical manual to perform the required preventative maintenance. This detailed set of written work instructions was in the form of an attachment which was issued with the maintenance work order. When this maintenance was subsequently performed, it was done using the developed set of detailed 92022S02~ | ||
This detailed set of written work instructions was in the form of an attachment which was issued with the maintenance work order.When this maintenance was subsequently performed, it was done using the developed set of detailed 92022S02~25i 91012~ | an FPL Group company 25i OCK 91012~ | ||
In addition, this maintenance was performed under the supervision of the Instrument and Control supervisor and the System Engineer.FPL regrets any confusion caused by our response of April 13, 1990.A detailed written procedure was issued on January 11, 1991, replacing the written instructions discussed above.Very tru y yours, J.H.Goldberg President | 05000735 ~go/ | ||
PDR /gp | |||
L-91-26 Page 2 instructions. In addition, this maintenance was performed under the supervision of the Instrument and Control supervisor and the System Engineer. | |||
FPL regrets any confusion caused by our response of April 13, 1990. | |||
A detailed written procedure was issued on January 11, 1991, replacing the written instructions discussed above. | |||
Very tru y yours, J. H. Goldberg President Nuclear Division t4 JHG/ JWH cc: Stewart D. Ebneter, Regional Administrator, USNRC Region IZ Senior Resident Inspector, USNRC, St. Lucie Plant}} | |||
Revision as of 21:48, 29 October 2019
| ML17223B066 | |
| Person / Time | |
|---|---|
| Site: | Saint Lucie |
| Issue date: | 01/24/1991 |
| From: | Goldberg J FLORIDA POWER & LIGHT CO. |
| To: | NRC OFFICE OF INFORMATION RESOURCES MANAGEMENT (IRM) |
| References | |
| L-91-26, NUDOCS 9101280251 | |
| Download: ML17223B066 (4) | |
Text
t 6 ACCELERATED DIjRIBUTION DEMONSTiTION SYSTEM REGULATORY INFORMATION DISTRIBUTION SYSTEM (RIDS)
ESSION NBR: 9101280251 DOC. DATE: 91/01/26 NOTARIZED: NO DOCKET FACIL:50-335 St. Lucie Plant., Unit 1, Florida Power & Light Co. 05000335 50-389 St. Lucie Plant, Unit 2, Florida Power & Light Co. 05000389 AUTH. NAME AUTHOR AFFILIATION GOLDBERG,J.'H. Florida Power & Light Co.
RECIP.NAME RECIPIENT AFFILIATION Document Control Branch (Document Control Desk)
SUM'ECT: Clarifies 900413 response to violations noted in Insp Repts 50-335/90-02 & 50-389/90-02.Corrective actions:nuclear job planning sys changed to include speed governor oil changes consistent w/vendor recommendations.
DISTRIBUTION CODE: ZE01D COPIES RECEIVED:LTR ENCL SIZE:
TITLE: General (50 Dkt)-Insp Rept/Notice of Vio ation Response NOTES:
RECIPIENT COPIES RECIPIENT COPIES ID CODE/NAME LTTR ENCL ID CODE/NAME LTTR ENCL PD2-2 PD NORRIS,J INTERNAL: ACRS 2 AEOD 1 AEOD/DEIIB 1 AEOD/TPAB 1 DEDRO 1 NRR MORISSEAU,D 1 NRR SHANKMAN,S 1 NRR/DLPQ/LPEB10 1 NRR/DOEA/OEAB 1 NRR/DREP/PEPB9 D 1 NRR/DRIS/DIR 1 - NRR/DST/DIR 8E2 1 NRR/PMAS/ILRB12 1 NUDOCS-ABSTRACT 1 OE DI 1 OGC/HDS2 ib RE ~FILE 0 1 RGN2 FILE 01 1 EXTERNAL: EG&G/BRYCE ~ J. H. NRC PDR NSZC NOTE TO ALL "RIDS" RECIPIENTS:
PLEASE HELP US TO REDUCE WASTE! CONTACT THE DOCUMENT CONTROL DESK, ROOM P 1-37 (EXT. 20079) TO ELliVIINATEYOUR NAME FROM DISTRIBUTION LISTS FOR DOCUMENTS YOU DON'T NEED!
TOTAL NUMBER OF COPIES REQUIRED: LTTR 24 ENCL Q
P.O. Box14000, Juno Beach, FL 33408-0420 JANUARY 2 4 1991 L-91-26 U. S. Nuclear Regulatory Commission Attn: Document Control Desk Washington, D. C. 20555 Gentlemen:
Re: St. Lucie Unit 1 and 2 Docket Nos. 50-335 and 50-389 Response to Notice of Violation Clarification Ins ection Re ort 90-02 Reference A: St. Lucie Unit 1 and 2 Docket Nos. 50-335 and 50-389 Response to Notice of Violation Ins ection Re ort 90-02 L-90-138, dated April 13, 1990 On January 10, 1991, a discussion between NRC Region II personnel NRC for and the St. Lucie Plant staff resulted in a request by the clarification of the "specific procedures" mentioned in Finding B, Response 3, in Reference A. In Reference A, Florida Power & Light Company (FPL) stated:
- 3. The specific vendor recommendation regarding the speed governor oil change was completed. The specific procedures
-
were changed to reflect the oil changes at a frequency consistent with the vendor's recommendation.
FPL submits the following clarification:
The Nuclear Job Planning System (NJPS) was changed to include the speed governor oil changes at a frequency consistent with the vendor's recommendation on February 2, 1990. The NJPS is a system designed to ensure preventative maintenance is scheduled within the desired time frames and tracked to completion.
A detailed set of written work instructions was developed using the guidance in the vendor technical manual to perform the required preventative maintenance. This detailed set of written work instructions was in the form of an attachment which was issued with the maintenance work order. When this maintenance was subsequently performed, it was done using the developed set of detailed 92022S02~
an FPL Group company 25i OCK 91012~
05000735 ~go/
PDR /gp
L-91-26 Page 2 instructions. In addition, this maintenance was performed under the supervision of the Instrument and Control supervisor and the System Engineer.
FPL regrets any confusion caused by our response of April 13, 1990.
A detailed written procedure was issued on January 11, 1991, replacing the written instructions discussed above.
Very tru y yours, J. H. Goldberg President Nuclear Division t4 JHG/ JWH cc: Stewart D. Ebneter, Regional Administrator, USNRC Region IZ Senior Resident Inspector, USNRC, St. Lucie Plant