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=Text=
=Text=
{{#Wiki_filter:ATTACHMENT D: 's IW tH s'a~'swv ROCHESTER GAS AHO ELECTRIC CORPORATION
{{#Wiki_filter:ATTACHMENT D                 :
~~~e<<v~89 EAST AVENUE, ROCHESTER, N.Y.14649 ,p"4 r.':4 (rR'I I~c, sRf 5 I wfmT Cl.f~<<0<<C>>ca Coat~s 546 2700 January 15, 1982 Director of Nuclear Reactor Regulation Attention:
                                                                                                    ~ ~ ~ e<<v
Mr.Dennis M.Crutchfield, Chief Operating Reactors Branch No.5 Division of Licensing U.S.Nuclear Regulatory Commission Washington, D.C.20555  
        's         IW tH s
      ' a~ 'swv ROCHESTER GAS AHO ELECTRIC CORPORATION                   ~ 89 EAST AVENUE, ROCHESTER, N.Y. 14649
,p"4 r. ':4 (rR                                                                         Cl.f ~ <<0<<C
'I I ~c, sRf 5 I wfmT                                                           >>ca Coat   ~ s 546 2700 January 15, 1982 Director of                 Nuclear Reactor Regulation Attention:                 Mr. Dennis M. Crutchfield, Chief Division of Operating Reactors Branch No. 5 Licensing
                                                                              /
                                                                            /Mj
                                                                                ~ .."
U.S. Nuclear Regulatory Commission                                         (f)
Washington, D.C. 20555                                                                 ":,' .'..
                                                                                              ~
                                                                                                    "


==Subject:==
==Subject:==
Steam Generator Sleeving R.E.Ginna~guclear Power Plant, Unit Docket No~PS5'"g4'4'~
Steam Generator         Sleeving R. E. Ginna~guclear Power Plant, Unit Docket   No~ PS5'"g4'4'~
<<~.<<se<<r  
                                        << .<<se<<r
                                          ~


==Dear Mr.Crutchfield:==
==Dear Mr.               Crutchfield:==


/~.."/Mj (f)":,'~.'.." Since August, 1980 Rochester Gas and Electric has had a steam generator sleeving development program.The purpose of this program has been to provide an alternative tube repair technique to plugging.Five (5)test sleeves were installed in the B Steam Generator at Ginna during November, 1980.An additional sixteen (16)sleeves were installed during the Spring 1981 refueling outage.The operating experience to date with these installations has been favorable.
Since August, 1980 Rochester Gas and Electric has had a steam generator sleeving development program.                             The purpose of this program has been to provide an alternative tube repair technique to plugging. Five (5) test sleeves were installed in the B Steam Generator at Ginna during November, 1980. An additional sixteen (16) sleeves were installed during the Spring 1981 refueling outage.                       The operating experience to date with these installations has been favorable. These installations are described in 'reports submitted to you by our letters dated November 6, 1980 and April 23, 1981.
These installations are described in'reports submitted to you by our letters dated November 6, 1980 and April 23, 1981.Our sleeving development program will be completed in the near future.The final sleeve design and installation procedures will be slightly different than previously described.
Our sleeving development program                   will be completed in the near       future.           The final sleeve design and installation                 procedures will be             slightly different than previously described.                       We are now planning on implementation of this sleeving technique as a standard steam generator tube repair procedure.                               In addition, we intend to preventatively sleeve several hundred sleeves in each steam geneiator over the next several years.                             This preventative sleeving program is scheduled to begin during our Spring 1982 refueling outage.                   It     is planned .to continue this preventative sleeving program during each steam'enerator inspection until all tubes potentially subject to degradation are completed.
We are now planning on implementation of this sleeving technique as a standard steam generator tube repair procedure.
At the present time, the Ginna Inservice Inspection Program limits           the maximum number of sleeves which may be installed                                         QO~
In addition, we intend to preventatively sleeve several hundred sleeves in each steam geneiator over the next several years.This preventative sleeving program is scheduled to begin during our Spring 1982 refueling outage.It is planned.to continue this preventative sleeving program during each steam'enerator inspection until all tubes potentially subject to degradation are completed.
during each steam generator inspection to 25 per steam generator.
At the present time, the Ginna Inservice Inspection Program limits the maximum number of sleeves which may be installed QO~during each steam generator inspection to 25 per steam generator.
In order to implement the sleeving program outlined above, a proposed change to the Inservice Inspection Program is enclosed.
In order to implement the sleeving program outlined above, a proposed change to the Inservice Inspection Program is enclosed.This change deletes the 25 sleeve limitation.
This change deletes the 25 sleeve limitation. No other changes are included in this revision. The provisions regarding inspection 8201200585       820.iS" Va~aCX-OEOOO2O4 8                     PDR I
No other changes are included in this revision.The provisions regarding inspection 8201200585 820.iS" Va~aCX-OEOOO2O4 8 PDR I January 15, 1982 Mr.Dennis M.Crutchfield and acceptable wall thickness of tubes and tube/sleeve combi-nations remain as previously approved.To facilitate your review'and approval of this proposed change to the Ginna Station Inservice Inspection Program, and in accordance with requests from members of your staff, it is proposed that an independent Design Review Board be used.The format and procedures for this board would be similar to those used for.the meeting of the San Onofre Unit 1 Steam Generator Sleeving Review'Board during October, 1980.A report describing the final details of our sleeve design and qualification program will be submitted to you on or about February 19, 1982.It is proposed that a Design Review Board meeting for the Ginna sleeving program be conducted on or about March 10, 1982 in Rochester.
 
Actual sleeve installation during the upcoming refueling outage at Ginna is not scheduled to commence until after April 20, 1982.With your concurrence, Rochester Gas and Electric will proceed to select participants for the board and establish the meeting arrangements and procedures.
January 15, 1982 Mr. Dennis M. Crutchfield and acceptable wall thickness of tubes and tube/sleeve combi-nations remain as previously approved.
We would like to review the pro-posed participants and arrangements with you in the near future.Very truly yours, John E.Maier  
To facilitate your review 'and approval of this proposed change to the Ginna Station Inservice Inspection Program, and in accordance with requests from members of your staff,   it is proposed that an independent Design Review Board be used. The format and procedures for this board would be similar to those used for .the meeting of the San Onofre Unit 1 Steam Generator Sleeving Review'Board during October, 1980. A report describing the final details of our sleeve design and qualification program will be submitted to you on or about February 19, 1982. It is proposed that a Design Review Board meeting for the Ginna sleeving program be conducted on or about March 10, 1982 in Rochester.
~ATTACHMENT D we<<0 Vl eW ROCHESTER CAS AHD ELECTRIC CORPORATION
Actual sleeve installation during the upcoming refueling outage at Ginna is not scheduled to commence until after April 20, 1982.
~89 EAST AVEHVE, ROCHESTER, H.Y.I4649.O~h K.'~i I ER (i (~%f 5 I~Ev, Cit+<<O~C'i~ca coac~~~540 2~00 January 1'5,.1982 Director of Nuclear Reactor Regulation Attention:
With your concurrence, Rochester Gas and Electric will proceed to select participants for the board and establish the meeting arrangements and procedures. We would like to review the pro-posed participants and arrangements with you in the near future.
Mr.Dennis M.Crutchfield, Ch'ief Operating Reactors Branch No.5 Division of Licensing U.S.Nuclear Regulatory Commission Washington, D.C.20555  
Very truly yours, John E. Maier
 
                  ~                           ATTACHMENT D
                                                                                                              <<0 Vl eW we ROCHESTER CAS AHD ELECTRIC CORPORATION                     ~ 89 EAST AVEHVE, ROCHESTER, H.Y. I4649
.O~h K. '~i I ER                                                                                     Cit+<<O~C (i ( ~ %f 5 I ~Ev,                                                                       'i~ca coac ~~~ 540 2 00
                                                                                                                  ~
January 1'5, .1982 Director of             Nuclear Reactor Regulation Attention:             Mr. Dennis M. Crutchfield, Ch'ief Operating Reactors Branch No. 5 Division of             Licensing U.S. Nuclear Regulatory Commission Washington, D.C. 20555


==Subject:==
==Subject:==
Steam Generator Sleeving R.E.Ginna Duel.ear Power Plant, Unit Docket No~I'-844'ear Mr.Crutchfield:
Steam Generator Sleeving R. E. Ginna Duel.ear Power               Plant, Unit Docket   No~I'-844'ear Mr.       Crutchfield:
Since August, 1980 Rochester Gas and Electric has had a steam generator sleeving development program.The purpose of this program has been to provide an alternative tube repair technique to plugging.Five (5)test sleeves were installed in the B Steam Generator at Ginna during November, 1980.An additional sixteen (16)sleeves were installed during the Spring 1981 refueling outage.The operating experience to date with these installations has been favorable.
Since August, 1980 Rochester Gas and Electric has had a steam generator sleeving development program. The purpose of this program has been to provide an alternative tube repair technique to plugging. Five (5) test sleeves were installed in the B Steam Generator at Ginna during November, 1980. An additional sixteen (16) sleeves were installed during the Spring 1981 refueling outage.                           The operating experience to date with these installations has been favorable. These installations are described in reports submitted to you by our letters dated November 6, 1980 and April 23, 1981.
These installations are described in reports submitted to you by our letters dated November 6, 1980 and April 23, 1981.Our sleeving development program will be completed in the near future.The final sleeve design and installation procedures will be slightly different than previously described.
Our sleeving development program                         will be completed in the near future.             The               final sleeve design and installation procedures will be slightly different than previously described. We are now planning on implementation of this sleeving technique as a standard steam generator tube repair procedure. Zn addition, we intend to preventatively sleeve several. hundred sleeves in each steam generator over the next several years.                                           This preventative sleeving program is scheduled to begin during our Spring 1982 refueling outage. Zt is planned .to continue this preventative sleeving program during each steam generator. inspection until all tubes potentially subject to,degradation are                             completed.'t the present time, the Ginna Znservice Inspection Program limits the           maximum number of sleeves which may be installed                                                       0 during each steam generator inspection to 25 per steam generator.                                                         s In order to implement the sleeving program outlined above, a proposed change to the Znservice Inspection Program is enclosed .
We are now planning on implementation of this sleeving technique as a standard steam generator tube repair procedure.
This change deletes the 25 sleeve limitation. No other. changes are included in this revision. The. provisions regarding inspection
Zn addition, we intend to preventatively sleeve several.hundred sleeves in each steam generator over the next several years.This preventative sleeving program is scheduled to begin during our Spring 1982 refueling outage.Zt is planned.to continue this preventative sleeving program during each steam generator.
 
inspection until all tubes potentially subject to,degradation are completed.'t the present time, the Ginna Znservice Inspection Program limits the maximum number of sleeves which may be installed 0 during each steam generator inspection to 25 per steam generator.
January, 15, 1982 Mr. Dennis M. Crutchfield and acceptable   wall thickness of tubes and,tube/sleeve combi-nations remain as previously approved.
s In order to implement the sleeving program outlined above, a proposed change to the Znservice Inspection Program is enclosed.This change deletes the 25 sleeve limitation.
To facilitate your review 'and approval of this proposed change to the Ginna Station Inservice Inspection Program, and in
No other.changes are included in this revision.The.provisions regarding inspection January, 15, 1982 Mr.Dennis M.Crutchfield and acceptable wall thickness of tubes and,tube/sleeve combi-nations remain as previously approved.To facilitate your review'and approval of this proposed change to the Ginna Station Inservice Inspection Program, and in accordance with requests from members of your staff, it is~proposed that an independent Design Review Board be used.The~format and procedures for this board would be similar to those used for the meeting of the San Onofre Unit 1 Steam Generator Sleeving Review'Board during October, 1980.A report describing the final details of our sleeve design and qualification program will be submitted to you on or about February 19, 1982.It is proposed that a Design Review Board meeting for the Ginna sleeving program be conducted on or about March 10, 1982 in Rochester..
  ~
Actual sleeve installation during the upcoming refueling outage at Ginna is not scheduled to commence until after April 20, 1982.With your concurrence, Rochester Gas and Electric will proceed to select participants for the board and establish the meeting arrangements and procedures.
accordance with requests from members of your staff, proposed that an independent Design Review   Board be it used.
Ne would like to review the pro-posed participants and arrangements with you in the near.future.Very truly yours, l]John E.Maier REGULlAT I VFORhlATION DiISTRIBUTION~(STE&#xc3;(RIDS)ACCKSSIOV NBR: S201200585 DOCKS DATE: S2/01/15 NQIT'ARIZED:
is The
NO DQCKEIT" tii'ACIL:50-244 Rboert>>Emmet Giinna Nuclear Pl anti Uni ti li Rochester..
~
O'I 05000244'UTH
format and procedures for this board would be similar to those used for the meeting of the San Onofre Unit 1 Steam Generator Sleeving Review'Board during October, 1980. A report describing the final details of our sleeve design and qualification program will be submitted to you on or about February 19, 1982. It is proposed that a Design Review Board meeting for the Ginna sleeving program be conducted on or about March 10, 1982 in Rochester..
~IV A'4IE>>AUT"NOR AFF>>ILII ATION MAIERi J.E'Rolches ter>>Gas L El ec t ri c Corp~RECIP~VAillE>>RECIIPIIEN>>Tl AFFILIIATIOV CRUTCHFIIELDiD
Actual sleeve installation during the upcoming refueling outage at Ginna is not scheduled to commence until after April 20, 1982.
~" 0'oer at jng Reactors Bra'nch 5-*i  
With your concurrence, Rochester Gas and Electric will proceed to select participants for the board and establish the meeting arrangements and procedures. Ne would like to review the pro-posed participants and arrangements with you in the near .future.
Very truly   yours, l]
John E. Maier
 
REGULlAT         I VFORhlATION DiISTRIBUTION~(STE&#xc3; (RIDS)
ACCKSSIOV NBR: S201200585                         DOCKS DATE:   S2/01/15 NQIT'ARIZED: NO                       DQCKEIT"     tii
  'ACIL:50-244 Rboert>> Emmet                     Giinna Nuclear Pl anti Uni ti AUT"NOR AFF>>ILIIATION li   Rochester.. O'I 05000244'UTH
        ~ IV A'4IE>>
MAIERiJ.E'                     Rolches ter>> Gas L El ec         t ri c Corp ~
RECIP ~ VAillE>>               RECIIPIIEN>>Tl     AFFILIIATIOV CRUTCHFIIELDiD~"                     0'oer at jng Reactors Bra'nch 5-
* i


==SUBJECT:==
==SUBJECT:==
F'orwa'r ds Revision>>, 6 to.A'pp 8 oif QA manuai'li for~inservice.
F'orwa'r ds Revision>>,           6   to. A'pp 8 oif QA manuai'li     for inservice.
insp orogra'm orovi ding al ternati ve repaii r for tube plugging techn'jque'.Sleevjng program scheduled fo.r imolementation durin'g Sar.jng 19S2 refueling outage.DISTRIBUTION:
                                                                                            ~
COOEI: ASSIS CDRiIES RECEIVED:LITR l>.IICLI j SIZE".P j~TITLE: General'i str i'outi op>>for af ter Issue'nce of Operating LIi cense IVOTES: 1.cosy:SKP>>S'acts~, LUr'..05000244'ECiIPII E>>ViTA ID CQDK>>/,VARKl ACTION: ORB tii5', SC!01.I>>VTERNALl:
insp orogra'm orovi ding al ternati ve repaii r for tube plugging techn'jque'.Sleevjng program scheduled fo.r imolementation DISTRIBUTION:
ELO NRA/DHF8 DEPIYOS i I R'" 04'O~IES LlT>>TR KiVC Ll 13 13 1 0 1 1 1.0 1 1 RKC'I PIER Tl ID>>i CODE'/4'ALKI IE 06 iVRR/DLl DIR.NR R'/0 S I/R'ABf COPIES LlTTR ENCLl 2 2 1 1 KXTERi4ALi:
TITLE:
ACRS NRC PQR IVT'I S 09 02 10 10 1 1>>1 LPOR iVS I Ci 03 05l'3C 3$TOTALI iilURBER Ori CI ORERSEIIIU'IRED; I ITTR 3jl5 ENCLI  
durin'g Sar.jng 19S2 refueling outage.
'ql, 1<I 4 1I H~1'" l' v"j/SIRE////////I I///////awt rK'.,-.: ROCHESTER GAS AND ELECTRIC CORPORATION o 89 EAST AVENUE, ROCHESTER, N.Y.14649 JOHN E.MA IER VICE PRESIDENT TCLCPHOMC ARCA CODC 7ld 546-2700 January 15, 1982 Director of Nuclear Reactor Regulation Attention:
COOEI:S'actsASSIS General'i str i'outi op>> for af ter CDRiIES RECEIVED:LITR            l > .IICLI Issue'nce of Operating j    SIZE".P j~
Mr.Dennis M.Crutchfield, Chief Operating Reactors Branch No.5 Division of Licensing U.S.Nuclear Regulatory Commission Washington, D.C.20555  
LIi cense IVOTES: 1. cosy:SKP>>                     , LUr'..                                                               05000244' ECiIPII E>>ViTA                                       RKC'I PIER Tl          COPIES ID CQDK>>/,VARKl               LlT>>TR KiVC Ll          ID>>i CODE'/ 4'ALKI      LlTTR ENCLl ACTION:         ORB     tii5', SC!       01.       13      13 04'O~IES I>>VTERNALl: ELO                                      1        0      IE                06        2      2 i
R
                          '"
NRA/DHF8 DEPIYOS I
1 1.
1 1
0 1
iVRR/DLl DIR.
NR R'/0 S I /R'ABf 1       1 KXTERi4ALi: ACRS                         09      10        10      LPOR                03 NRC PQR                   02        1                iVS  I Ci          05l IVT'I S                             1>>       1
                                                                    '3C               3$
TOTALI iilURBER Ori               CI ORERSEIIIU'IRED;     I ITTR   3jl5   ENCLI
 
                  'ql, 1
        <I 4 1I H
~1'" l'
 
v
      /SIRE     ////////I "j
I/// //// awt rK'.,-.:
ROCHESTER GAS AND ELECTRIC CORPORATION o 89 EAST AVENUE, ROCHESTER, N.Y. 14649 JOHN E. MA IER                                                               TCLCPHOMC VICE PRESIDENT                                                       ARCA CODC 7ld 546-2700 January 15, 1982 Director of                 Nuclear Reactor Regulation Attention:                   Mr. Dennis M. Crutchfield, Chief Operating Reactors Branch No. 5 Division of                 Licensing U.S. Nuclear Regulatory Commission Washington, D.C. 20555


==Subject:==
==Subject:==
Steam Generator Sleeving R.E.Ginna Nuclear Power Plant, Unit Docket, No.50-244  
Steam Generator Sleeving R. E. Ginna Nuclear Power   Plant, Unit Docket, No. 50-244
 
==Dear Mr.                Crutchfield:==
 
Since August, 1980 Rochester Gas and Electric has had a steam generator sleeving development program. The purpose of this program has been to provide an alternative tube repair technique to plugging. Five (5) test sleeves were installed in the B Steam Generator at Ginna during November, 1980. An additional sixteen (16) sleeves were installed during the Spring 1981 refueling outage.                    The operating experience to date with these installations has been favorable. These installations are described in reports submitted to you by our letters dated November 6, 1980 and April 23, 1981.
Our          sleeving development program will be completed in the near future.                  The final sleeve          and installation procedures will be slightly different than design            previously described. We are now planning on implementation of this sleeving technique as a standard steam generator tube repair procedure. In addition, we intend to preventatively sleeve several hundred sleeves in each steam generator over the next several years.                    This preventative sleeving program is scheduled to begin during our Spring 1982 refueling outage. It is planned to continue this preventative sleeving program during each steam generator inspection until all tubes potentially subject to degradation are completed.
At the present time, the Ginna Inservice Inspection Program limits the maximum number of sleeves which may be installed                                  QO during each steam generator inspection to 25 per steam generator.
In order to implement the sleeving program outlined above, a proposed change to the Inservice Inspection Program is enclosed.
This change deletes the 25 sleeve limitation. No other changes are included in this revision. The provisions regarding inspection 820i200585      820i5    ~l PDR ADOCK    08000244 I,    8                  PDR
 
4 J


==Dear Mr.Crutchfield:==
ROCHESTER GAS AND ELECTRIC CORP.
4            SHEET NO.
DpTE      January 15, 1982 TO        Mr. Dennis M. Crutchfield and acceptable    wall thickness of tubes and tube/sleeve combi-nations remain as previously approved.
To facilitate your review and approval of this proposed change to the Ginna Station Inservice Inspection Program, and in accordance with requests from members of your staff,      it proposed that an independent Design Review Board be used. The is format and procedures for this board would be similar to those used for the meeting of the San Onofre Unit 1 Steam Generator Sleeving Review Board during October, 1980. A report describing
  'the final details of our sleeve design and qualification program will be submitted to you on or about February 19, 1982. It is proposed that a Design Review Board meeting for the Ginna sleeving program be conducted on or about March 10, 1982 in Rochester.
Actual sleeve installation during the upcoming refueling outage at Ginna is not scheduled to commence until after April 20, 1982.
With your concurrence, Rochester Gas and Electric will proceed to select participants for the board and establish the meeting arrangements and procedures.      We would like to review the pro-posed participants and arrangements with you in the near future.
Very truly yours, Jo  E. Maier


Since August, 1980 Rochester Gas and Electric has had a steam generator sleeving development program.The purpose of this program has been to provide an alternative tube repair technique to plugging.Five (5)test sleeves were installed in the B Steam Generator at Ginna during November, 1980.An additional sixteen (16)sleeves were installed during the Spring 1981 refueling outage.The operating experience to date with these installations has been favorable.
r J
These installations are described in reports submitted to you by our letters dated November 6, 1980 and April 23, 1981.Our sleeving development program will be completed in the near future.The final sleeve design and installation procedures will be slightly different than previously described.
E}}
We are now planning on implementation of this sleeving technique as a standard steam generator tube repair procedure.
In addition, we intend to preventatively sleeve several hundred sleeves in each steam generator over the next several years.This preventative sleeving program is scheduled to begin during our Spring 1982 refueling outage.It is planned to continue this preventative sleeving program during each steam generator inspection until all tubes potentially subject to degradation are completed.
At the present time, the Ginna Inservice Inspection Program limits the maximum number of sleeves which may be installed QO during each steam generator inspection to 25 per steam generator.
In order to implement the sleeving program outlined above, a proposed change to the Inservice Inspection Program is enclosed.This change deletes the 25 sleeve limitation.
No other changes are included in this revision.The provisions regarding inspection 820i200585 820i5~l PDR ADOCK 08000244 I, 8 PDR 4 J ROCHESTER GAS AND ELECTRIC CORP.DpTE January 15, 1982 TO Mr.Dennis M.Crutchfield 4 SHEET NO.and acceptable wall thickness of tubes and tube/sleeve combi-nations remain as previously approved.To facilitate your review and approval of this proposed change to the Ginna Station Inservice Inspection Program, and in accordance with requests from members of your staff, it is proposed that an independent Design Review Board be used.The format and procedures for this board would be similar to those used for the meeting of the San Onofre Unit 1 Steam Generator Sleeving Review Board during October, 1980.A report describing
'the final details of our sleeve design and qualification program will be submitted to you on or about February 19, 1982.It is proposed that a Design Review Board meeting for the Ginna sleeving program be conducted on or about March 10, 1982 in Rochester.
Actual sleeve installation during the upcoming refueling outage at Ginna is not scheduled to commence until after April 20, 1982.With your concurrence, Rochester Gas and Electric will proceed to select participants for the board and establish the meeting arrangements and procedures.
We would like to review the pro-posed participants and arrangements with you in the near future.Very truly yours, Jo E.Maier r E J}}

Revision as of 08:53, 29 October 2019

Forwards Revision 6 to App B of QA Manual for Inservice Insp Program Providing Alternative Repair for Tube Plugging Technique.Sleeving Program Scheduled for Implementation During Spring 1982 Refueling Outage
ML17309A215
Person / Time
Site: Ginna Constellation icon.png
Issue date: 01/15/1982
From: Maier J
ROCHESTER GAS & ELECTRIC CORP.
To: Crutchfield D
Office of Nuclear Reactor Regulation
Shared Package
ML17258A459 List:
References
NUDOCS 8201200585
Download: ML17309A215 (10)


Text

ATTACHMENT D  :

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'I I ~c, sRf 5 I wfmT >>ca Coat ~ s 546 2700 January 15, 1982 Director of Nuclear Reactor Regulation Attention: Mr. Dennis M. Crutchfield, Chief Division of Operating Reactors Branch No. 5 Licensing

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U.S. Nuclear Regulatory Commission (f)

Washington, D.C. 20555 ":,' .'..

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Subject:

Steam Generator Sleeving R. E. Ginna~guclear Power Plant, Unit Docket No~ PS5'"g4'4'~

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Dear Mr. Crutchfield:

Since August, 1980 Rochester Gas and Electric has had a steam generator sleeving development program. The purpose of this program has been to provide an alternative tube repair technique to plugging. Five (5) test sleeves were installed in the B Steam Generator at Ginna during November, 1980. An additional sixteen (16) sleeves were installed during the Spring 1981 refueling outage. The operating experience to date with these installations has been favorable. These installations are described in 'reports submitted to you by our letters dated November 6, 1980 and April 23, 1981.

Our sleeving development program will be completed in the near future. The final sleeve design and installation procedures will be slightly different than previously described. We are now planning on implementation of this sleeving technique as a standard steam generator tube repair procedure. In addition, we intend to preventatively sleeve several hundred sleeves in each steam geneiator over the next several years. This preventative sleeving program is scheduled to begin during our Spring 1982 refueling outage. It is planned .to continue this preventative sleeving program during each steam'enerator inspection until all tubes potentially subject to degradation are completed.

At the present time, the Ginna Inservice Inspection Program limits the maximum number of sleeves which may be installed QO~

during each steam generator inspection to 25 per steam generator.

In order to implement the sleeving program outlined above, a proposed change to the Inservice Inspection Program is enclosed.

This change deletes the 25 sleeve limitation. No other changes are included in this revision. The provisions regarding inspection 8201200585 820.iS" Va~aCX-OEOOO2O4 8 PDR I

January 15, 1982 Mr. Dennis M. Crutchfield and acceptable wall thickness of tubes and tube/sleeve combi-nations remain as previously approved.

To facilitate your review 'and approval of this proposed change to the Ginna Station Inservice Inspection Program, and in accordance with requests from members of your staff, it is proposed that an independent Design Review Board be used. The format and procedures for this board would be similar to those used for .the meeting of the San Onofre Unit 1 Steam Generator Sleeving Review'Board during October, 1980. A report describing the final details of our sleeve design and qualification program will be submitted to you on or about February 19, 1982. It is proposed that a Design Review Board meeting for the Ginna sleeving program be conducted on or about March 10, 1982 in Rochester.

Actual sleeve installation during the upcoming refueling outage at Ginna is not scheduled to commence until after April 20, 1982.

With your concurrence, Rochester Gas and Electric will proceed to select participants for the board and establish the meeting arrangements and procedures. We would like to review the pro-posed participants and arrangements with you in the near future.

Very truly yours, John E. Maier

~ ATTACHMENT D

<<0 Vl eW we ROCHESTER CAS AHD ELECTRIC CORPORATION ~ 89 EAST AVEHVE, ROCHESTER, H.Y. I4649

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January 1'5, .1982 Director of Nuclear Reactor Regulation Attention: Mr. Dennis M. Crutchfield, Ch'ief Operating Reactors Branch No. 5 Division of Licensing U.S. Nuclear Regulatory Commission Washington, D.C. 20555

Subject:

Steam Generator Sleeving R. E. Ginna Duel.ear Power Plant, Unit Docket No~I'-844'ear Mr. Crutchfield:

Since August, 1980 Rochester Gas and Electric has had a steam generator sleeving development program. The purpose of this program has been to provide an alternative tube repair technique to plugging. Five (5) test sleeves were installed in the B Steam Generator at Ginna during November, 1980. An additional sixteen (16) sleeves were installed during the Spring 1981 refueling outage. The operating experience to date with these installations has been favorable. These installations are described in reports submitted to you by our letters dated November 6, 1980 and April 23, 1981.

Our sleeving development program will be completed in the near future. The final sleeve design and installation procedures will be slightly different than previously described. We are now planning on implementation of this sleeving technique as a standard steam generator tube repair procedure. Zn addition, we intend to preventatively sleeve several. hundred sleeves in each steam generator over the next several years. This preventative sleeving program is scheduled to begin during our Spring 1982 refueling outage. Zt is planned .to continue this preventative sleeving program during each steam generator. inspection until all tubes potentially subject to,degradation are completed.'t the present time, the Ginna Znservice Inspection Program limits the maximum number of sleeves which may be installed 0 during each steam generator inspection to 25 per steam generator. s In order to implement the sleeving program outlined above, a proposed change to the Znservice Inspection Program is enclosed .

This change deletes the 25 sleeve limitation. No other. changes are included in this revision. The. provisions regarding inspection

January, 15, 1982 Mr. Dennis M. Crutchfield and acceptable wall thickness of tubes and,tube/sleeve combi-nations remain as previously approved.

To facilitate your review 'and approval of this proposed change to the Ginna Station Inservice Inspection Program, and in

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accordance with requests from members of your staff, proposed that an independent Design Review Board be it used.

is The

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format and procedures for this board would be similar to those used for the meeting of the San Onofre Unit 1 Steam Generator Sleeving Review'Board during October, 1980. A report describing the final details of our sleeve design and qualification program will be submitted to you on or about February 19, 1982. It is proposed that a Design Review Board meeting for the Ginna sleeving program be conducted on or about March 10, 1982 in Rochester..

Actual sleeve installation during the upcoming refueling outage at Ginna is not scheduled to commence until after April 20, 1982.

With your concurrence, Rochester Gas and Electric will proceed to select participants for the board and establish the meeting arrangements and procedures. Ne would like to review the pro-posed participants and arrangements with you in the near .future.

Very truly yours, l]

John E. Maier

REGULlAT I VFORhlATION DiISTRIBUTION~(STEÃ (RIDS)

ACCKSSIOV NBR: S201200585 DOCKS DATE: S2/01/15 NQIT'ARIZED: NO DQCKEIT" tii

'ACIL:50-244 Rboert>> Emmet Giinna Nuclear Pl anti Uni ti AUT"NOR AFF>>ILIIATION li Rochester.. O'I 05000244'UTH

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RECIP ~ VAillE>> RECIIPIIEN>>Tl AFFILIIATIOV CRUTCHFIIELDiD~" 0'oer at jng Reactors Bra'nch 5-

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SUBJECT:

F'orwa'r ds Revision>>, 6 to. A'pp 8 oif QA manuai'li for inservice.

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insp orogra'm orovi ding al ternati ve repaii r for tube plugging techn'jque'.Sleevjng program scheduled fo.r imolementation DISTRIBUTION:

TITLE:

durin'g Sar.jng 19S2 refueling outage.

COOEI:S'actsASSIS General'i str i'outi op>> for af ter CDRiIES RECEIVED:LITR l > .IICLI Issue'nce of Operating j SIZE".P j~

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ROCHESTER GAS AND ELECTRIC CORPORATION o 89 EAST AVENUE, ROCHESTER, N.Y. 14649 JOHN E. MA IER TCLCPHOMC VICE PRESIDENT ARCA CODC 7ld 546-2700 January 15, 1982 Director of Nuclear Reactor Regulation Attention: Mr. Dennis M. Crutchfield, Chief Operating Reactors Branch No. 5 Division of Licensing U.S. Nuclear Regulatory Commission Washington, D.C. 20555

Subject:

Steam Generator Sleeving R. E. Ginna Nuclear Power Plant, Unit Docket, No. 50-244

Dear Mr. Crutchfield:

Since August, 1980 Rochester Gas and Electric has had a steam generator sleeving development program. The purpose of this program has been to provide an alternative tube repair technique to plugging. Five (5) test sleeves were installed in the B Steam Generator at Ginna during November, 1980. An additional sixteen (16) sleeves were installed during the Spring 1981 refueling outage. The operating experience to date with these installations has been favorable. These installations are described in reports submitted to you by our letters dated November 6, 1980 and April 23, 1981.

Our sleeving development program will be completed in the near future. The final sleeve and installation procedures will be slightly different than design previously described. We are now planning on implementation of this sleeving technique as a standard steam generator tube repair procedure. In addition, we intend to preventatively sleeve several hundred sleeves in each steam generator over the next several years. This preventative sleeving program is scheduled to begin during our Spring 1982 refueling outage. It is planned to continue this preventative sleeving program during each steam generator inspection until all tubes potentially subject to degradation are completed.

At the present time, the Ginna Inservice Inspection Program limits the maximum number of sleeves which may be installed QO during each steam generator inspection to 25 per steam generator.

In order to implement the sleeving program outlined above, a proposed change to the Inservice Inspection Program is enclosed.

This change deletes the 25 sleeve limitation. No other changes are included in this revision. The provisions regarding inspection 820i200585 820i5 ~l PDR ADOCK 08000244 I, 8 PDR

4 J

ROCHESTER GAS AND ELECTRIC CORP.

4 SHEET NO.

DpTE January 15, 1982 TO Mr. Dennis M. Crutchfield and acceptable wall thickness of tubes and tube/sleeve combi-nations remain as previously approved.

To facilitate your review and approval of this proposed change to the Ginna Station Inservice Inspection Program, and in accordance with requests from members of your staff, it proposed that an independent Design Review Board be used. The is format and procedures for this board would be similar to those used for the meeting of the San Onofre Unit 1 Steam Generator Sleeving Review Board during October, 1980. A report describing

'the final details of our sleeve design and qualification program will be submitted to you on or about February 19, 1982. It is proposed that a Design Review Board meeting for the Ginna sleeving program be conducted on or about March 10, 1982 in Rochester.

Actual sleeve installation during the upcoming refueling outage at Ginna is not scheduled to commence until after April 20, 1982.

With your concurrence, Rochester Gas and Electric will proceed to select participants for the board and establish the meeting arrangements and procedures. We would like to review the pro-posed participants and arrangements with you in the near future.

Very truly yours, Jo E. Maier

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