ML18052A258: Difference between revisions
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-PALISADES PLANT - | ** | ||
STEAM GENERATOR INSERVICE INSPECTION REPORT | * Power company General Offices: 1945 West Parnell Ro11d, Jackson, Ml 49201 * (517) 788-0550 | ||
30, 1985 when the final tube plugging occurred. | / | ||
A total of eight (8) tubes,;.were plugged following the inspection; all were located in "B" Steam Generator:"* (see Attachment 5 for details). | January 27, 1986 | ||
The number of tubes plugged does not the assumptions or change the safety analysis. ,I " It is Consumers Power Company's belief that the str1'cf *adherence to secondary water .purity limits and maintaining the secondary s'a:de of the steam generators in wet lay-up, as much as possible, during conditions has limited tube corrosion. | ; | ||
The results of 1985 show, essentially, no further degradation of the "A" or "B" steam tul;>ing occurred during the last operating cycle. | \ | ||
L Kuemin -Staff Licensing Engineer CC Administrator, Region III, USNRC NRC Resident Inspector | \ | ||
-Palisades | Director, Nuclear Reactor Regulation US Nuclear Regulatory Commission Washington, DC 20555 DOCKET 50-255 - LICENSE DPR~20 - PALISADES PLANT - | ||
*ea02030153 860127 | ~1985 STEAM GENERATOR INSERVICE INSPECTION REPORT In accordance with P~lisades Technical Specificatiq'.n 4.14.6, the enclosed Steam Generator Inseivice Inspection Report is sub~itted. | ||
The inspection occurred from December 1 to December.' 30, 1985 when the final tube plugging occurred. A total of eight (8) tubes,;.were plugged following the inspection; all were located in "B" Steam Generator:"* (see Attachment 5 for details). The number of tubes plugged does not vJoi~te the assumptions or change the safety analysis. ,I " | |||
It is Consumers Power Company's belief that the str1'cf *adherence to secondary water .purity limits and maintaining the secondary s'a:de of the steam generators in wet lay-up, as much as possible, during non-oper~ting conditions has limited tube corrosion. The results of 1985 inspec~ion show, essentially, no further degradation of the "A" or "B" steam generat~r tul;>ing occurred during the last operating cycle. | |||
o~?f.~ | |||
~ames L Kuemin - | |||
Staff Licensing Engineer CC Administrator, Region III, USNRC NRC Resident Inspector - Palisades | |||
*ea02030153 860127 PDR G | |||
ADOCK 05000255 PDR ! | |||
. | |||
w*. | |||
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. | |||
* | |||
'1* | |||
I | |||
". | |||
OC0186-0012-NL02}} | |||
Revision as of 19:41, 21 October 2019
| ML18052A258 | |
| Person / Time | |
|---|---|
| Site: | Palisades |
| Issue date: | 01/27/1986 |
| From: | Kuemin J CONSUMERS ENERGY CO. (FORMERLY CONSUMERS POWER CO.) |
| To: | Office of Nuclear Reactor Regulation |
| Shared Package | |
| ML18052A259 | List: |
| References | |
| NUDOCS 8602030153 | |
| Download: ML18052A258 (1) | |
Text
consumers
- Power company General Offices: 1945 West Parnell Ro11d, Jackson, Ml 49201 * (517) 788-0550
/
January 27, 1986
\
\
Director, Nuclear Reactor Regulation US Nuclear Regulatory Commission Washington, DC 20555 DOCKET 50-255 - LICENSE DPR~20 - PALISADES PLANT -
~1985 STEAM GENERATOR INSERVICE INSPECTION REPORT In accordance with P~lisades Technical Specificatiq'.n 4.14.6, the enclosed Steam Generator Inseivice Inspection Report is sub~itted.
The inspection occurred from December 1 to December.' 30, 1985 when the final tube plugging occurred. A total of eight (8) tubes,;.were plugged following the inspection; all were located in "B" Steam Generator:"* (see Attachment 5 for details). The number of tubes plugged does not vJoi~te the assumptions or change the safety analysis. ,I "
It is Consumers Power Company's belief that the str1'cf *adherence to secondary water .purity limits and maintaining the secondary s'a:de of the steam generators in wet lay-up, as much as possible, during non-oper~ting conditions has limited tube corrosion. The results of 1985 inspec~ion show, essentially, no further degradation of the "A" or "B" steam generat~r tul;>ing occurred during the last operating cycle.
o~?f.~
~ames L Kuemin -
Staff Licensing Engineer CC Administrator, Region III, USNRC NRC Resident Inspector - Palisades
- ea02030153 860127 PDR G
ADOCK 05000255 PDR !
.
w*.
-(
.
'1*
I
".
OC0186-0012-NL02