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{{#Wiki_filter:e Public Service Electric and Gas Company P.O. Box E Hancocks Bridge, New Jersey 08038 Salem Generating Station May 11, 1990 U.S. Nuclear Regulatory Commission Document Control Desk Washington, DC 20555  
{{#Wiki_filter:e OPS~G Public Service Electric and Gas Company P.O. Box E Hancocks Bridge, New Jersey 08038 Salem Generating Station May 11, 1990 U.S. Nuclear Regulatory Commission Document Control Desk Washington, DC               20555


==Dear Sir:==
==Dear Sir:==
MONTHLY OPERATING REPORT SALEM NO. 1 DOCKET NO. 50-272 In compliance with Section 6.9.1.6, Reporting Requirements for the Salem Technical Specifications, the original copy of the monthly operating reports for the month of April 1990 are being sent to you. RH:pc Average Daily Unit Power Level Operating Data Report Unit Shutdowns and Power Reductions Safety Related Maintenance Major Plant Modifications Operating Summary Refueling Information Sincerely
 
: yours, L. K. Miller General Manager -Salem Operations cc: Mr. William T. Russell Regional Administrator USNRC Region I 631 Park Avenue King of Prussia, PA 19046 Enclosures 8-1-7.R4 The Energy People 95-2189 (11M)12-84 Month APRIL, 1990 Day Average Daily Power (MWe-NET) 1 0 2 0 3 0 4 0 5 0 6 0 7 122 8 890 9 587 10 0 11 0 12 0 13 0 14 0 15 0. 16 0 P. 8.1-7 Rl AVERAGE DAILY UNIT POWER LEVEL Level Docket No. Unit Name Date Completed by Telephone 50-272 Salem # 1 05-10-90 Art Orticelle 609-339-2122 Day Average Daily Power Level (MWe-NET) 17 0 18 0 19 0 20 0 21 0 22 0 23 0 24 0 25 0 26 0 27 0 28 0 29 0 30 0 31 OPERATING DATA REPORT Docket No: 50-272 Date: 05-10-90 Completed by: Art Orticelle Telephone:
MONTHLY OPERATING REPORT SALEM NO. 1 DOCKET NO. 50-272 In compliance with Section 6.9.1.6, Reporting Requirements for the Salem Technical Specifications, the original copy of the monthly operating reports for the month of April 1990 are being sent to you.
609-339-2122 Operating Status 1. Unit Name Salem No. 1 Notes 2. Reporting Period April 1990 3 . Licensed Thermal Power (MWt) 3411 4 . Nameplate Rating (Gross MWe) 1170 5. Design Electrical Rating (Net MWe) 1115 6. Maximum Dependable Capacity(Gross MWe) 1149 7. Maximum Dependable Capacity (Net MWe) 1106 8 . If Changes Occur in Capacity Ratings (items 3 through 7) since Last Report, Give Reason N/A 9. Power Level to Which Restricted, if any (Net MWe) N/A
Average Daily Unit Power Level Operating Data Report Unit Shutdowns and Power Reductions Safety Related Maintenance Major Plant Modifications Operating Summary Refueling Information Sincerely yours,
                                                        ;le~
L. K. Miller General Manager -
Salem Operations RH:pc cc:     Mr. William T. Russell Regional Administrator USNRC Region I 631 Park Avenue King of Prussia, PA               19046 Enclosures 8-1-7.R4 The Energy People 95-2189 (11M)12-84
 
AVERAGE DAILY UNIT POWER LEVEL Docket No. 50-272 Unit Name      Salem # 1 Date          05-10-90 Completed by  Art Orticelle Telephone      609-339-2122 Month    APRIL, 1990 Day Average Daily Power Level            Day Average Daily Power Level (MWe-NET)                                 (MWe-NET) 1          0                                17           0 2          0                               18           0 3          0                               19           0 4          0                                20           0 5          0                                21           0 6          0                                22           0 7        122                                23           0 8        890                                24           0 9        587                                25           0 10          0                                26           0 11          0                                27           0 12          0                               28           0 13          0                               29           0 14          0                               30           0 15          0.                              31 16          0 P. 8.1-7 Rl
 
OPERATING DATA REPORT Docket No:     50-272 Date:           05-10-90 Completed by:   Art Orticelle             Telephone:     609-339-2122 Operating Status
: 1. Unit Name                         Salem No. 1     Notes
: 2. Reporting Period                 April 1990
: 3. Licensed Thermal Power (MWt)             3411
: 4. Nameplate Rating (Gross MWe)             1170
: 5. Design Electrical Rating (Net MWe)       1115
: 6. Maximum Dependable Capacity(Gross MWe) 1149
: 7. Maximum Dependable Capacity (Net MWe)     1106
: 8. If Changes Occur in Capacity Ratings (items 3 through 7) since Last Report, Give Reason     N/A
: 9. Power Level to Which Restricted, if any (Net MWe)           N/A
                                                          --~~'-"------------
: 10. Reasons for Restrictions, if any --=-N'-'-/--=-A=----------------------
: 10. Reasons for Restrictions, if any --=-N'-'-/--=-A=----------------------
This Month Year to Date Cumulative
This Month     Year to Date   Cumulative
: 11. Hours in Reporting Period 719 2879 112512 12. No. of Hrs. Reactor was Critical 108.68 2162.68 73071.23 13. Reactor Reserve Shutdown Hrs. 0 0 0 14. Hours Generator On-Line 48.87 2102.79 70798.55 15. Unit Reserve Shutdown Hours 0 0 0 16. Gross Thermal Energy Generated (MWH) 134088.0 6892562.4 221993488.4
: 11. Hours in Reporting Period               719           2879       112512
: 17. Gross Elec. Energy Generated (MWH) 41440 2290760 73752120 18. Net Elec. Energy Generated (MWH) 26313 2203218 70214928 19. Unit Service Factor 6.8 73.0 62.9 20. Unit Availability Factor 6.8 73.0 62.9 21. Unit Capacity Factor (using MDC Net) 3.3 69.2 56.4 22. Unit Capacity Factor (using DER Net) 3.3 68.6 56.0 23. Unit Forced Outage Rate 93.2 27.0 21.6 24. Shutdowns scheduled over next 6 months (type, date and duration of each) Unit #1 Eighth Refueling scheduled on October 6, 1990 and lasting 45 da s. 25. If shutdown at end of Report Period, Estimated Date of Startup: Estimated start-up date of May 11, 1990. 8-1-7.R2 -----------------------
: 12. No. of Hrs. Reactor was Critical         108.68       2162.68     73071.23
--------------------------------------------------------------------
: 13. Reactor Reserve Shutdown Hrs.             0             0             0
NO. DATE 0033 4-01-90 0035 4-09-90 I I I 1 F: Forced S: Scheduled UNIT SHUTDOWN AND POWER REDUCTIONS REFDRI' MONTH APRIL 1990 OOCKEI' NO.:
: 14. Hours Generator On-Line                   48.87       2102.79     70798.55
___ _ UNIT NAME: Salem #1 DURATION TYPE 1 (HOURS} REASON 2 F 262.8 A F 513.5 A I 2 Reason: A-Equillll8nt Failure (Explain)
: 15. Unit Reserve Shutdown Hours               0             0             0
B-Maintenance or Test C-Refueling D-Regulatory Restriction MEI'HOD OF SHUITING OOWN REACIDR 4 3 E--Operator Training & Lic-ense Examination F-Admi.llistrati ve G--Operational Error (&'Plain)
: 16. Gross Thermal Energy Generated (MWH)                         134088.0     6892562.4   221993488.4
H-Other (Ex-plain)
: 17. Gross Elec. Energy Generated (MWH)                         41440       2290760     73752120
--------LICENSE EVENT SY STEN REFDRI' # CODE 4 ----IB ----CH 3 Method: 1-Manual 2-Manual Scram 3-Automatic Scram 4-Continuation of Previous outage 5-1.oad Reduction 9-0ther CD.'1PONENT CODE 5 INSTRU INSTRU DATE: 05-10-90 COMPLEI'ED BY: Art Orticelle TELEPHONE:
: 18. Net Elec. Energy Generated (MWH)       26313       2203218     70214928
339-2122 CAUSE AND CORRECTIVE ACTION 'ID PREVENT RECURRENCE 1A S.E.C. #12 S.G. FEED PUMP 4 5 Exhibit G -Instrnctions Exhibit 1 -Same for Preparation of Data Source Entry Sheets for Licensee Event Report (LER) File (NUREG-0161)
: 19. Unit Service Factor                       6.8           73.0         62.9
I I MAJOR MODIFICATIONS MdNTH: -APRIL 1990 *DCR lEC-02245 1EC-02251A lSC-2092 PRINCIPAL SYSTEM Reactor Coolant Smoke Detection Residual Heat Removal
: 20. Unit Availability Factor                   6.8           73.0         62.9
* Design Change Request DOCKET NO: UNIT NAME: DATE: COMPLETED BY: TELEPHONE:
: 21. Unit Capacity Factor (using MDC Net)                       3.3           69.2         56.4
50-272 SALEM 1 MAY 10, 1990 M. MORRONI (609) 339-2068 DESCRIPTION This design change replaced the 1/4 Reactor Coolant Pump (RCP} Breaker Open Anticipatory Trip signal above P-8 with a 2/4 RCP Breaker Open Anticipatory trip signal above P-7. This design change installed additional smoke detection equipment to various zones of the Auxiliary Building.
: 22. Unit Capacity Factor (using DER Net)                       3.3           68.6         56.0
This design change modified the control circuits for Valves RHl and RH2 to delete the auto closure interlock feature.
: 23. Unit Forced Outage Rate                   93.2           27.0         21.6
MiJ6R PLANT MODIFICATIONS MONTH: -APRIL 1990 DOCKET NO: UNIT NAME: 50-272 SALEM 1 *DCR lEC-02245 1EC-02251A lSC-2092 DATE: COMPLETED BY: TELEPHONE:
: 24. Shutdowns scheduled over next 6 months (type, date and duration of each)
SAFETY EVALUATION 10 CFR 50.59 MAY 10, 1990 M. MORRONI (609) 339-2068 This design change replaced the 1/4 Reactor Coolant Pump (RCP) Breaker Open Anticipatory Trip signal above P-8 with a 2/4 RCP Breaker Open Anticipatory trip signal above P-7. This design change reduces the potential for inadvertent Rx trips and challenges to the Reactor Protection System. There was no change to any plant process or discharge or to the environmental impact of the plant. No unreviewed safety or environmental questions are involved.
Unit #1 Eighth Refueling scheduled on October 6, 1990 and lasting 45 da s.
This design change installed additional smoke detection equipment to various zones of the Auxiliary Building.
: 25. If shutdown at end of Report Period, Estimated Date of Startup:
This provides additional coverage of equipment areas by the automatic detection system. There was no change to any plant process or discharge or to the environmental impact of the plant. No unreviewed safety or environmental questions are involved.
Estimated start-up date of May 11, 1990.
This design change modified the control circuits for Valves RHl and RH2 to delete the auto closure interlock feature. Elimination of this feature reduced the potential for inadvertant actuation of these valves and brought the system design in conformance with current requirements.
8-1-7.R2
There was no change to any plant process or discharge or to the environmental impact of the plant. No unreviewed safety or environmental questions are involved.  
 
*DCR -Design Change Request I I I ________ _J   
UNIT SHUTDOWN AND POWER REDUCTIONS                             OOCKEI' NO.: --'5'--"0--'-2"'--'7~2_ _ __
REFDRI' MONTH APRIL
                                                                            ---   1990
                                                                                    -----                                     UNIT NAME:     Salem #1 DATE:   05-10-90 COMPLEI'ED BY:   Art Orticelle TELEPHONE:     339-2122 MEI'HOD OF SHUITING      LICENSE DURATION                OOWN          EVENT        SYSTEN    CD.'1PONENT          CAUSE AND CORRECTIVE ACTION NO.      DATE    TYPE 1    (HOURS}      REASON 2  REACIDR        REFDRI' #    CODE 4    CODE  5                'ID PREVENT RECURRENCE 0033      4-01-90      F        262.8          A          4          ----            IB      INSTRU          1A S.E.C.
0035      4-09-90      F          513.5          A          3          ----            CH      INSTRU          #12 S.G. FEED PUMP I
I      I          I        I                                                                                                                                          I 1                2                                              3                      4                             5 F: Forced        Reason:                                        Method:                Exhibit G - Instrnctions     Exhibit 1 - Same S: Scheduled      A-Equillll8nt Failure (Explain)                1-Manual                for Preparation of Data       Source B-Maintenance or Test                          2-Manual Scram          Entry Sheets for Licensee C-Refueling                                      3-Automatic Scram      Event Report (LER) File D-Regulatory Restriction                        4-Continuation of      (NUREG-0161)
E--Operator Training &Lic-ense Examination        Previous outage F-Admi.llistrative                              5-1.oad Reduction G--Operational Error (&'Plain)                  9-0ther H-Other (Ex-plain)
 
MAJOR ~LANT MODIFICATIONS              DOCKET NO:   50-272 MdNTH: - APRIL 1990                    UNIT NAME:   SALEM 1 DATE: MAY 10, 1990 COMPLETED BY:  M. MORRONI TELEPHONE:  (609) 339-2068
    *DCR          PRINCIPAL SYSTEM          DESCRIPTION lEC-02245      Reactor Coolant  This design change replaced the 1/4 Reactor Coolant Pump (RCP} Breaker Open Anticipatory Trip signal above P-8 with a 2/4 RCP Breaker Open Anticipatory trip signal above P-7.
1EC-02251A    Smoke Detection  This design change installed additional smoke detection equipment to various zones of the Auxiliary Building.
lSC-2092      Residual Heat    This design change modified the Removal          control circuits for Valves RHl and RH2 to delete the auto closure interlock feature.
* Design Change Request
 
MiJ6R PLANT MODIFICATIONS                   DOCKET NO:  50-272 MONTH: - APRIL 1990                         UNIT NAME: SALEM 1 DATE: MAY 10, 1990 COMPLETED BY: M. MORRONI TELEPHONE: (609) 339-2068
    *DCR          SAFETY EVALUATION 10 CFR 50.59 lEC-02245        This design change replaced the 1/4 Reactor Coolant Pump (RCP) Breaker Open Anticipatory Trip signal above P-8 with a 2/4 RCP Breaker Open Anticipatory trip signal above P-7.
This design change reduces the potential for inadvertent Rx trips and challenges to the Reactor Protection System.
There was no change to any plant process or discharge or to the environmental impact of the plant. No unreviewed safety or environmental questions are involved.
1EC-02251A        This design change installed additional smoke detection equipment to various zones of the Auxiliary Building. This provides additional coverage of equipment areas by the automatic detection system. There was no change to any plant process or discharge or to the environmental impact of the plant. No unreviewed safety or environmental questions are involved.
lSC-2092          This design change modified the control circuits for Valves RHl and RH2 to delete the auto closure interlock feature.
Elimination of this feature reduced the potential for inadvertant actuation of these valves and brought the system design in conformance with current requirements.
There was no change to any plant process or discharge or to the environmental impact of the plant. No unreviewed safety or environmental questions are involved.
  *DCR - Design Change Request I
I I
_ _ _ _ _ _ _ _ _J
 
S~F~TY RELATED MAINTENANCE                    DOCKET NO:  50-272 MONTH: - APRIL 1990                          UNIT NAME:  SALEM 1 DATE:  MAY 10, 1990 COMPLETED BY: M. MORRON!
TELEPHONE:  (609) 339-2068 WO NO    UNIT                        EQUIPMENT IDENTIFICATION 890804101    1    13 SERVICE WATER PUMP FAILURE DESCRIPTION:  REMOVE AND REPLACE WITH SPARE PUMP 900104080    1    12 SAFETY INJECTION PUMP FLOW ORIFICE FAILURE DESCRIPTION:  ORIFICE FLANGE LEAKING - REPLACE GASKET 900309121    1    11SW127 FAILURE DESCRIPTION:  NO AUTO CONTROL - TROUBLESHOOT 900321100    1    14 SWITCHGEAR FAILURE DESCRIPTION:  EXHAUST FAN STOP INDICATION DOES NOT LIGHT - TROUBLESHOOT 900402122    1    15 CONTAINMENT FAN COIL UNIT FAILURE DESCRIPTION:      INDICATION PEGS AT LOW SPEED -
TROUBLESHOOT 900419103    1    #1 MAIN TRANSFORMER FAILURE DESCRIPTION:  TROUBLESHOOT GEOMAGNETIC INDUCTION COUNTERS


RELATED MAINTENANCE MONTH: -APRIL 1990 DOCKET NO: UNIT NAME: 50-272 SALEM 1 WO NO 890804101 900104080 900309121 900321100 900402122 900419103 UNIT 1 1 1 1 1 DATE: COMPLETED BY: TELEPHONE:
                                        ,
MAY 10, 1990 M. MORRON! (609) 339-2068 EQUIPMENT IDENTIFICATION 13 SERVICE WATER PUMP FAILURE DESCRIPTION:
I I
REMOVE AND REPLACE WITH SPARE PUMP 12 SAFETY INJECTION PUMP FLOW ORIFICE FAILURE DESCRIPTION:
SALEM GENERATING STATION MONTHLY OPERATING  
ORIFICE FLANGE LEAKING -REPLACE GASKET 11SW127 FAILURE DESCRIPTION:
NO AUTO CONTROL -TROUBLESHOOT 14 SWITCHGEAR FAILURE DESCRIPTION:
EXHAUST FAN STOP INDICATION DOES NOT LIGHT -TROUBLESHOOT 15 CONTAINMENT FAN COIL UNIT FAILURE DESCRIPTION:
INDICATION PEGS AT LOW SPEED -TROUBLESHOOT 1 #1 MAIN TRANSFORMER FAILURE DESCRIPTION:
TROUBLESHOOT GEOMAGNETIC INDUCTION COUNTERS 
,--------________ , I I SALEM UNIT NO. 1 SALEM GENERATING STATION MONTHLY OPERATING  


==SUMMARY==
==SUMMARY==
  -UNIT 1 APRIL 1990 The Unit entered the period shutdown for repairs to lA Safeguards Equipment Cabinet (SEC). Following repairs to the SEC, delays were encountered during heatup due to leakage from an Emergency Core Cooling System (ECCS) check valve. The valve was reseated and the Unit was restored to approximately 91% power on April 7, 1990. The Unit continued to operate at that level until April 9, 1990, when the reactor tripped following separation of the linkage on 12 Steam Generator Feed Pump which resulted in a low water level in 12 Steam Generator.
  - UNIT 1 APRIL 1990 SALEM UNIT NO. 1 The Unit entered the period shutdown for repairs to lA Safeguards Equipment Cabinet (SEC). Following repairs to the SEC, delays were encountered during heatup due to leakage from an Emergency Core Cooling System (ECCS) check valve. The valve was reseated and the Unit was restored to approximately 91% power on April 7, 1990. The Unit continued to operate at that level until April 9, 1990, when the reactor tripped following separation of the linkage on 12 Steam Generator Feed Pump which resulted in a low water level in 12 Steam Generator. The Unit remained shutdown through the rest of the period for ECCS full flow testing and correction of identified concerns.
The Unit remained shutdown through the rest of the period for ECCS full flow testing and correction of identified concerns.


INFORMATION MONTH: -APRIL 1990 MONTH APRIL 1990 DOCKET NO: UNIT NAME: DATE: COMPLETED BY: TELEPHONE:
R~FUELING INFORMATION                         DOCKET NO:  50-272 MONTH: - APRIL 1990                           UNIT NAME:   SALEM 1 DATE:   MAY 10, 1990 COMPLETED BY:   M. MORRON!
: 1. Refueling information has changed from last month: YES NO x 2. Scheduled date for next refueling:
TELEPHONE:   (609) 339-2068 MONTH APRIL 1990
October 6, 1990 50-272 SALEM 1 MAY 10, 1990 M. MORRON! (609) 339-2068 3. Scheduled date for restart following refueling:
: 1. Refueling information has changed from last month:
November 19, 1990 4. a) Will Technical Specification changes or other license amendments be required?:
YES                 NO   x
YES NO NOT DETERMINED TO DATE x b) Has the reload fuel design been reviewed by the Station Operating Review Committee?:
: 2. Scheduled date for next refueling:   October 6, 1990
YES NO x If no, when is it scheduled?:
: 3. Scheduled date for restart following refueling:   November 19, 1990
September 1990 5. Scheduled date(s) for submitting proposed licensing action: N/A 6. Important licensing considerations associated with refueling:
: 4. a) Will Technical Specification changes or other license amendments be required?:
YES                 NO NOT DETERMINED TO DATE   x b) Has the reload fuel design been reviewed by the Station Operating Review Committee?:
YES                 NO   x If no, when is it scheduled?:   September 1990
: 5. Scheduled date(s) for submitting proposed licensing action:
N/A
: 6. Important licensing considerations associated with refueling:
: 7. Number of Fuel Assemblies:
: 7. Number of Fuel Assemblies:
: a. Incore 193 b. In Spent Fuel Storage 540 8. Present licensed spent fuel storage capacity:
: a. Incore                                                       193
1170 Future spent fuel storage capacity:
: b. In Spent Fuel Storage                                         540
1170 9. Date of last refueling that can be discharged to the spent fuel pool assuming the present licensed capacity:
: 8. Present licensed spent fuel storage capacity:                     1170 Future spent fuel storage capacity:                               1170
September 2001 8-l-7.R4}}
: 9. Date of last refueling that can be discharged to the spent fuel pool assuming the present licensed capacity:                                       September 2001 8-l-7.R4}}

Revision as of 10:55, 21 October 2019

Monthly Operating Rept for Apr 1990 for Salem Unit 1.W/ 900511 Ltr
ML18095A200
Person / Time
Site: Salem PSEG icon.png
Issue date: 04/30/1990
From: Miller L, Orticelle A
Public Service Enterprise Group
To:
NRC OFFICE OF INFORMATION RESOURCES MANAGEMENT (IRM)
References
NUDOCS 9005180058
Download: ML18095A200 (9)


Text

e OPS~G Public Service Electric and Gas Company P.O. Box E Hancocks Bridge, New Jersey 08038 Salem Generating Station May 11, 1990 U.S. Nuclear Regulatory Commission Document Control Desk Washington, DC 20555

Dear Sir:

MONTHLY OPERATING REPORT SALEM NO. 1 DOCKET NO. 50-272 In compliance with Section 6.9.1.6, Reporting Requirements for the Salem Technical Specifications, the original copy of the monthly operating reports for the month of April 1990 are being sent to you.

Average Daily Unit Power Level Operating Data Report Unit Shutdowns and Power Reductions Safety Related Maintenance Major Plant Modifications Operating Summary Refueling Information Sincerely yours,

le~

L. K. Miller General Manager -

Salem Operations RH:pc cc: Mr. William T. Russell Regional Administrator USNRC Region I 631 Park Avenue King of Prussia, PA 19046 Enclosures 8-1-7.R4 The Energy People 95-2189 (11M)12-84

AVERAGE DAILY UNIT POWER LEVEL Docket No. 50-272 Unit Name Salem # 1 Date 05-10-90 Completed by Art Orticelle Telephone 609-339-2122 Month APRIL, 1990 Day Average Daily Power Level Day Average Daily Power Level (MWe-NET) (MWe-NET) 1 0 17 0 2 0 18 0 3 0 19 0 4 0 20 0 5 0 21 0 6 0 22 0 7 122 23 0 8 890 24 0 9 587 25 0 10 0 26 0 11 0 27 0 12 0 28 0 13 0 29 0 14 0 30 0 15 0. 31 16 0 P. 8.1-7 Rl

OPERATING DATA REPORT Docket No: 50-272 Date: 05-10-90 Completed by: Art Orticelle Telephone: 609-339-2122 Operating Status

1. Unit Name Salem No. 1 Notes
2. Reporting Period April 1990
3. Licensed Thermal Power (MWt) 3411
4. Nameplate Rating (Gross MWe) 1170
5. Design Electrical Rating (Net MWe) 1115
6. Maximum Dependable Capacity(Gross MWe) 1149
7. Maximum Dependable Capacity (Net MWe) 1106
8. If Changes Occur in Capacity Ratings (items 3 through 7) since Last Report, Give Reason N/A
9. Power Level to Which Restricted, if any (Net MWe) N/A

--~~'-"------------

10. Reasons for Restrictions, if any --=-N'-'-/--=-A=----------------------

This Month Year to Date Cumulative

11. Hours in Reporting Period 719 2879 112512
12. No. of Hrs. Reactor was Critical 108.68 2162.68 73071.23
13. Reactor Reserve Shutdown Hrs. 0 0 0
14. Hours Generator On-Line 48.87 2102.79 70798.55
15. Unit Reserve Shutdown Hours 0 0 0
16. Gross Thermal Energy Generated (MWH) 134088.0 6892562.4 221993488.4
17. Gross Elec. Energy Generated (MWH) 41440 2290760 73752120
18. Net Elec. Energy Generated (MWH) 26313 2203218 70214928
19. Unit Service Factor 6.8 73.0 62.9
20. Unit Availability Factor 6.8 73.0 62.9
21. Unit Capacity Factor (using MDC Net) 3.3 69.2 56.4
22. Unit Capacity Factor (using DER Net) 3.3 68.6 56.0
23. Unit Forced Outage Rate 93.2 27.0 21.6
24. Shutdowns scheduled over next 6 months (type, date and duration of each)

Unit #1 Eighth Refueling scheduled on October 6, 1990 and lasting 45 da s.

25. If shutdown at end of Report Period, Estimated Date of Startup:

Estimated start-up date of May 11, 1990.

8-1-7.R2

UNIT SHUTDOWN AND POWER REDUCTIONS OOCKEI' NO.: --'5'--"0--'-2"'--'7~2_ _ __

REFDRI' MONTH APRIL

--- 1990


UNIT NAME: Salem #1 DATE: 05-10-90 COMPLEI'ED BY: Art Orticelle TELEPHONE: 339-2122 MEI'HOD OF SHUITING LICENSE DURATION OOWN EVENT SYSTEN CD.'1PONENT CAUSE AND CORRECTIVE ACTION NO. DATE TYPE 1 (HOURS} REASON 2 REACIDR REFDRI' # CODE 4 CODE 5 'ID PREVENT RECURRENCE 0033 4-01-90 F 262.8 A 4 ---- IB INSTRU 1A S.E.C. 0035 4-09-90 F 513.5 A 3 ---- CH INSTRU #12 S.G. FEED PUMP I

I I I I I 1 2 3 4 5 F: Forced Reason: Method: Exhibit G - Instrnctions Exhibit 1 - Same S: Scheduled A-Equillll8nt Failure (Explain) 1-Manual for Preparation of Data Source B-Maintenance or Test 2-Manual Scram Entry Sheets for Licensee C-Refueling 3-Automatic Scram Event Report (LER) File D-Regulatory Restriction 4-Continuation of (NUREG-0161)

E--Operator Training &Lic-ense Examination Previous outage F-Admi.llistrative 5-1.oad Reduction G--Operational Error (&'Plain) 9-0ther H-Other (Ex-plain)

MAJOR ~LANT MODIFICATIONS DOCKET NO: 50-272 MdNTH: - APRIL 1990 UNIT NAME: SALEM 1 DATE: MAY 10, 1990 COMPLETED BY: M. MORRONI TELEPHONE: (609) 339-2068

  • DCR PRINCIPAL SYSTEM DESCRIPTION lEC-02245 Reactor Coolant This design change replaced the 1/4 Reactor Coolant Pump (RCP} Breaker Open Anticipatory Trip signal above P-8 with a 2/4 RCP Breaker Open Anticipatory trip signal above P-7.

1EC-02251A Smoke Detection This design change installed additional smoke detection equipment to various zones of the Auxiliary Building.

lSC-2092 Residual Heat This design change modified the Removal control circuits for Valves RHl and RH2 to delete the auto closure interlock feature.

  • Design Change Request

MiJ6R PLANT MODIFICATIONS DOCKET NO: 50-272 MONTH: - APRIL 1990 UNIT NAME: SALEM 1 DATE: MAY 10, 1990 COMPLETED BY: M. MORRONI TELEPHONE: (609) 339-2068

  • DCR SAFETY EVALUATION 10 CFR 50.59 lEC-02245 This design change replaced the 1/4 Reactor Coolant Pump (RCP) Breaker Open Anticipatory Trip signal above P-8 with a 2/4 RCP Breaker Open Anticipatory trip signal above P-7.

This design change reduces the potential for inadvertent Rx trips and challenges to the Reactor Protection System.

There was no change to any plant process or discharge or to the environmental impact of the plant. No unreviewed safety or environmental questions are involved.

1EC-02251A This design change installed additional smoke detection equipment to various zones of the Auxiliary Building. This provides additional coverage of equipment areas by the automatic detection system. There was no change to any plant process or discharge or to the environmental impact of the plant. No unreviewed safety or environmental questions are involved.

lSC-2092 This design change modified the control circuits for Valves RHl and RH2 to delete the auto closure interlock feature.

Elimination of this feature reduced the potential for inadvertant actuation of these valves and brought the system design in conformance with current requirements.

There was no change to any plant process or discharge or to the environmental impact of the plant. No unreviewed safety or environmental questions are involved.

  • DCR - Design Change Request I

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S~F~TY RELATED MAINTENANCE DOCKET NO: 50-272 MONTH: - APRIL 1990 UNIT NAME: SALEM 1 DATE: MAY 10, 1990 COMPLETED BY: M. MORRON!

TELEPHONE: (609) 339-2068 WO NO UNIT EQUIPMENT IDENTIFICATION 890804101 1 13 SERVICE WATER PUMP FAILURE DESCRIPTION: REMOVE AND REPLACE WITH SPARE PUMP 900104080 1 12 SAFETY INJECTION PUMP FLOW ORIFICE FAILURE DESCRIPTION: ORIFICE FLANGE LEAKING - REPLACE GASKET 900309121 1 11SW127 FAILURE DESCRIPTION: NO AUTO CONTROL - TROUBLESHOOT 900321100 1 14 SWITCHGEAR FAILURE DESCRIPTION: EXHAUST FAN STOP INDICATION DOES NOT LIGHT - TROUBLESHOOT 900402122 1 15 CONTAINMENT FAN COIL UNIT FAILURE DESCRIPTION: INDICATION PEGS AT LOW SPEED -

TROUBLESHOOT 900419103 1 #1 MAIN TRANSFORMER FAILURE DESCRIPTION: TROUBLESHOOT GEOMAGNETIC INDUCTION COUNTERS

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SALEM GENERATING STATION MONTHLY OPERATING

SUMMARY

- UNIT 1 APRIL 1990 SALEM UNIT NO. 1 The Unit entered the period shutdown for repairs to lA Safeguards Equipment Cabinet (SEC). Following repairs to the SEC, delays were encountered during heatup due to leakage from an Emergency Core Cooling System (ECCS) check valve. The valve was reseated and the Unit was restored to approximately 91% power on April 7, 1990. The Unit continued to operate at that level until April 9, 1990, when the reactor tripped following separation of the linkage on 12 Steam Generator Feed Pump which resulted in a low water level in 12 Steam Generator. The Unit remained shutdown through the rest of the period for ECCS full flow testing and correction of identified concerns.

R~FUELING INFORMATION DOCKET NO: 50-272 MONTH: - APRIL 1990 UNIT NAME: SALEM 1 DATE: MAY 10, 1990 COMPLETED BY: M. MORRON!

TELEPHONE: (609) 339-2068 MONTH APRIL 1990

1. Refueling information has changed from last month:

YES NO x

2. Scheduled date for next refueling: October 6, 1990
3. Scheduled date for restart following refueling: November 19, 1990
4. a) Will Technical Specification changes or other license amendments be required?:

YES NO NOT DETERMINED TO DATE x b) Has the reload fuel design been reviewed by the Station Operating Review Committee?:

YES NO x If no, when is it scheduled?: September 1990

5. Scheduled date(s) for submitting proposed licensing action:

N/A

6. Important licensing considerations associated with refueling:
7. Number of Fuel Assemblies:
a. Incore 193
b. In Spent Fuel Storage 540
8. Present licensed spent fuel storage capacity: 1170 Future spent fuel storage capacity: 1170
9. Date of last refueling that can be discharged to the spent fuel pool assuming the present licensed capacity: September 2001 8-l-7.R4