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See also: [[followed by::IR 05000280/1989034]]


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{{#Wiki_filter:-. VIRGINIA ELECTRIC AND POWER COMPANY RICHMOND, VIRGINIA 23261 February 6, 1990 United States Nuclear Regulatory  
{{#Wiki_filter:-. VIRGINIA ELECTRIC AND POWER COMPANY RICHMOND, VIRGINIA 23261 February 6, 1990 United States Nuclear Regulatory Commission Attention:
Commission  
Document Control Desk Washington, D.C. 20555 Gentlemen:
Attention:  
Document Control Desk Washington, D.C. 20555 Gentlemen:  
VIRGINIA ELECTRIC AND POWER COMPANY SORRY POWER STATION UNITS 1 AND 2 REPLY TO A NOTICE OF VIOLATION  
VIRGINIA ELECTRIC AND POWER COMPANY SORRY POWER STATION UNITS 1 AND 2 REPLY TO A NOTICE OF VIOLATION  
-Ser_i al No. NL/RPC Docket Nos. License Nos. NRC INSPECTION  
-Ser_i al No. NL/RPC Docket Nos. License Nos. NRC INSPECTION REPORT NOS. 50-280/89-34 AND 50-281/89-34 89-880 R3 50-280 50-281 . DPR-32 DPR-37 We have reviewed your letter dated December 22, 1989, in reference to the NRC inspection conducted-on October 29 -November 25, 1989, for Surry Power Station. The inspection was reported in Inspection Report Nos! 50-280/89-34 and 50-281/89-34.
REPORT NOS. 50-280/89-34  
Our response to the violations described in the Notice of Violation is provided in Attachment
AND 50-281/89-34  
: 1. Your letter expressed concern over the material condition of the process monitoring instrumentation.
89-880 R3 50-280 50-281 . DPR-32 DPR-37 We have reviewed your letter dated December 22, 1989, in reference  
You requested that we address our program to assure that process monitoring equipment is maintained operable and outline specific actions being taken to return inoperable process instrumentation to service in an expeditious manner.* -Operability of the process monitoring instrumentation is demonstrated periodically through the station's surveillance and testing program. If a component is found to be inoperable, alternative measures are employed to monitor the parameter in accordance with Technical Specifications and a.station deviation is submitted.
to the NRC inspection  
On December 21, 1989, a station deviation trending report was submitted to the Chairman of the Station Nuclear Safety Operating Committee (SNSOC), which discussed recurring problems with process radiation monitors.
conducted-
To more fully address these issues, the SNSOC established a subcommittee composed of senior technical staff members. The subcommittee has been tasked to review process radiation monitoring operations data sources, including equipment operability history, and to submit a report on its findings by February 28, 1990. 6ased on this report, SNSOC will assign further actions as appropriate.
on October 29 -November 25, 1989, for Surry Power Station. The inspection  
We are keeping the NRC Resident Inspectors informed of the progress and results of this review. The project to replace and return _the component cooling water (CCW) heat exchanger service water effluent monitors to operation is being implemented in conjunction with the ongoing project to replace the CCW heat exchangers.
was reported in Inspection  
One. of the four installed heat exchangers has been replaced and the installation of the associated service water effluent monitor is scheduled for completion in February 1990, subject to receipt of the remaining equipment.
Report Nos! 50-280/89-34  
The next two CCW heat exchangers are scheduled for replacement during the Unit I ref~jPel~;/
and 50-281/89-34.  
9002220547 900206 PDR ADOCK 05000280 I,., Q PNV The final CCW heat The alternative remain in effect outage currently planned for the fourth quarter of 1990. exchanger is scheduled for the second quarter of 1991. sampling measures specified by Technical Specifications will until completion of the project. In a telephone conversation between Mr. S. Shaeffer of the NRC Region II staff and Mr. D. Sommers of my staff, an extension of 15 days was granted for our reply to this Notice of Violation.
Our response to the violations  
We have no objection to this inspection report being made a matter of public disclosure.
described  
in the Notice of Violation  
is provided in Attachment  
1. Your letter expressed  
concern over the material condition  
of the process monitoring  
instrumentation.  
You requested  
that we address our program to assure that process monitoring  
equipment  
is maintained  
operable and outline specific actions being taken to return inoperable  
process instrumentation  
to service in an expeditious  
manner.* -Operability  
of the process monitoring  
instrumentation  
is demonstrated  
periodically  
through the station's  
surveillance  
and testing program. If a component  
is found to be inoperable, alternative  
measures are employed to monitor the parameter  
in accordance  
with Technical  
Specifications  
and a.station  
deviation  
is submitted.  
On December 21, 1989, a station deviation  
trending report was submitted  
to the Chairman of the Station Nuclear Safety Operating  
Committee (SNSOC), which discussed  
recurring  
problems with process radiation  
monitors.  
To more fully address these issues, the SNSOC established  
a subcommittee  
composed of senior technical  
staff members. The subcommittee  
has been tasked to review process radiation  
monitoring  
operations  
data sources, including  
equipment  
operability  
history, and to submit a report on its findings by February 28, 1990. 6ased on this report, SNSOC will assign further actions as appropriate.  
We are keeping the NRC Resident Inspectors  
informed of the progress and results of this review. The project to replace and return _the component  
cooling water (CCW) heat exchanger  
service water effluent monitors to operation  
is being implemented  
in conjunction  
with the ongoing project to replace the CCW heat exchangers.  
One. of the four installed  
heat exchangers  
has been replaced and the installation  
of the associated  
service water effluent monitor is scheduled  
for completion  
in February 1990, subject to receipt of the remaining  
equipment.  
The next two CCW heat exchangers  
are scheduled  
for replacement  
during the Unit I ref~jPel~;/  
9002220547  
900206 PDR ADOCK 05000280 I,., Q PNV
The final CCW heat The alternative  
remain in effect outage currently  
planned for the fourth quarter of 1990. exchanger  
is scheduled  
for the second quarter of 1991. sampling measures specified  
by Technical  
Specifications  
will until completion  
of the project. In a telephone  
conversation  
between Mr. S. Shaeffer of the NRC Region II staff and Mr. D. Sommers of my staff, an extension  
of 15 days was granted for our reply to this Notice of Violation.  
We have no objection  
to this inspection  
report being made a matter of public disclosure.  
Should you have .any further questions, please contact us. Very truly yours, &\-S~ W. L. Stewart Senior Vice President  
Should you have .any further questions, please contact us. Very truly yours, &\-S~ W. L. Stewart Senior Vice President  
-Nuclear Attachment  
-Nuclear Attachment cc: U.S. Nuclear Regulatory Commission Region II 101 Marietta Street, N.W. Suite 2900 , Atlanta, Georgia 30323 Mr. W. E. Holland NRC Senior Resident Inspector Surry Power Station --------, I NRC Comment ATTACHMENT 1 REPLY TO A NOTICE OF VIOLATION REPORTED DORING THE NRC INSPECTIONS ON OCTOBER 29 -NOVtMBER 25, 1989 INSPECTION REPORT NOS. 50-280/89-34 AND 50-281/89-34 During the Nuclear Regulatory Commission (NRC) inspection conducted on October 29 -November 25, 1989, violations of NRC requirements were identified.
cc: U.S. Nuclear Regulatory  
In accordance with the '.'General Statement of Policy and Procedure for NRC Enforcement Actions, 11 10 CFR Part 2, Appendix C ( 1989), the violations are listed below:
Commission  
* A. 10 CFR 50, Appendix B, Criteriori V, requires that activities affecting quality shall be prescribed by documented instructions or procedures appropriate to the circumstances.
Region II 101 Marietta Street, N.W. Suite 2900 , Atlanta, Georgia 30323 Mr. W. E. Holland NRC Senior Resident Inspector  
Contrary to the above, activities affecting quality were not prescribed by adequate instructions and/or procedures, in that: 1. Operating Procedure, 2-0P-1.3, Unit Startup Operation (350/450 to HSD), Revision dated June 14, 1989, did not adequately caution the operators to maintain specific pressure control prior to testing reactor coolant system accumulator discharge valves. On November 21, 1989, during Unit 2 startu~, operators allowed the reactor coolant system pressure to eiceed 1000 psig, prior to cipening and de-energizing the accumulator discharge isolation valve motor operators, a violation of Technical . Specification 3.3.A.10.
Surry Power Station --------, I
: 2. On November 13, 1989, a resin waste transfer evolution was conducted without adequate*
NRC Comment ATTACHMENT  
procedure control resulting in three licensee employees being contaminated when a pipe cap was removed from a pressurized system; 3. On approximately October 25, 1989, the Unit 2 flood control dikes, which protect against flooding of the service water supply motor control valves to the recirculation spray heat exchangers, were removed with inadequate modification and operation procedure control resulttng in heatup of the unit above 350°F, on November 6 and 20, 1989, with inoperable recirculation spray systems, a violation of Technical Specification 3.4. This violation has been. categorized as a Severity Level IV violation (Supplement I) for Unit 2. B. 10 CFR 50, Appendix B, Criterion VII, requires that measures and controls shall be established to prevent the use of incorrect or defective material, parts, and components.
1 REPLY TO A NOTICE OF VIOLATION  
REPORTED DORING THE NRC INSPECTIONS  
ON OCTOBER 29 -NOVtMBER 25, 1989 INSPECTION  
REPORT NOS. 50-280/89-34  
AND 50-281/89-34  
During the Nuclear Regulatory  
Commission (NRC) inspection  
conducted  
on October 29 -November 25, 1989, violations  
of NRC requirements  
were identified.  
In accordance  
with the '.'General  
Statement  
of Policy and Procedure  
for NRC Enforcement  
Actions, 11 10 CFR Part 2, Appendix C ( 1989), the violations  
are listed below: * A. 10 CFR 50, Appendix B, Criteriori  
V, requires that activities  
affecting  
quality shall be prescribed  
by documented  
instructions  
or procedures  
appropriate  
to the circumstances.  
Contrary to the above, activities  
affecting  
quality were not prescribed  
by adequate instructions  
and/or procedures, in that: 1. Operating  
Procedure, 2-0P-1.3, Unit Startup Operation  
(350/450 to HSD), Revision dated June 14, 1989, did not adequately  
caution the operators  
to maintain specific pressure control prior to testing reactor coolant system accumulator  
discharge  
valves. On November 21, 1989, during Unit 2 startu~, operators  
allowed the reactor coolant system pressure to eiceed 1000 psig, prior to cipening and de-energizing  
the accumulator  
discharge  
isolation  
valve motor operators, a violation  
of Technical . Specification  
3.3.A.10.  
2. On November 13, 1989, a resin waste transfer evolution  
was conducted  
without adequate*  
procedure  
control resulting  
in three licensee employees  
being contaminated  
when a pipe cap was removed from a pressurized  
system; 3. On approximately  
October 25, 1989, the Unit 2 flood control dikes, which protect against flooding of the service water supply motor control valves to the recirculation  
spray heat exchangers, were removed with inadequate  
modification  
and operation  
procedure  
control resulttng  
in heatup of the unit above 350°F, on November 6 and 20, 1989, with inoperable  
recirculation  
spray systems, a violation  
of Technical  
Specification  
3.4. This violation  
has been. categorized  
as a Severity Level IV violation (Supplement  
I) for Unit 2. B. 10 CFR 50, Appendix B, Criterion  
VII, requires that measures and controls shall be established  
to prevent the use of incorrect  
or defective  
material, parts, and components.  
1 of 11   
1 of 11   
** * Contrary to . the above, adequate measures were not established  
**
to prevent incorrect  
* Contrary to . the above, adequate measures were not established to prevent incorrect gaskets from being installed in components in that: 1. Work Order 87218, dated October 28, 1989, identified that an incorrect gasket had been installed in. safety injection check valve 2""'.SI-79 during the previous outage. This condition had contributed to a failure of the valve,to properly seat during subsequent unit operation.
gaskets from being installed  
: 2. Inspection of safety injection check valve 2-SI-91 in accordance with Engineering Work -Request 89-6848, dated November 3, 1989, indicated that an incorrect gasket had been installed during the previous outage. 3. After interim corrective action was conducted for examples 1 and 2 above on November 1, 1989, incorrect gaskets were installed in a Unit 2 pressurizer safety valve on November 14, 1989, and subsequent review revealed potential incorrect gaskets in the Unit 1 pressurizer safety valves. This violation has been categorized as a Severity Level IV violation  
in components  
.(Supplement I) for Units 1 and 2. C.
in that: 1. Work Order 87218, dated October 28, 1989, identified  
* Technical Specification 3.7, Table 3.7.5(a) requires that grab samples be collected and analyzed at least once per 12 hours whenever radioactive liquid effluent monitoring instrumentation is out of service. Contrary to the above, grab* samples were not collected and analyzed at least once per 12 hours in that, on August 2, 1989, samples for the Component cooling service water effluent line were collected and analyzed 30 minutes outside the required 12-hour timeframe.
that an incorrect  
This violation has been categorized as a Severity Level IV violation (Supplement I) for Units 1 and 2. 2 of 11 ~.;-;-:
gasket had been installed  
* RESPONSE TO NOTICE OF VIOLATION . INSPECTION REPORT NOS. 50-280/89-34 AND 50-281/89-34 A. 10CFR50, Appendix B, Criterion V, requires that activities affecting quality shall be prescribed by documented instructions or procedures appropriate to the circumstances  
in. safety injection  
.. Contrary to the above, activities affecting quality were not prescribed by adequate instructions and/or procedures, in that: 1. Operating procedure, 2-0P-1.3, Unit Startup Operation (350/450 to HSD), Revision dated June 14, 1989, did not adequately caution the operators to maintain specific pressure control prior to testing reactor coolant system accumulator discharge valves. On November 21, 1989, during Unit 2 startup, operators allowed the reactor coolant system pressure to exceed 1000 psig, prior to opening and de-energizing the accumulator discharge isolation valve motor operators, a violation of Technical*
check valve 2""'.SI-79  
Specification 3.3.A.10.
during the previous outage. This condition  
(1) ADMISSION OR DENIAL OF THE ALLEGED VIOLATION:
had contributed  
The violation is correct as stated. (2) REASON FOR VIOLATION Upon completion of OP-7.1.1 (Leak Testing Accumulator Check Valves), the electricians were directed.to reinstall the seal-in contacts for the motor operated accumulator discharge valves. While waiting fof this step to be completed, the operations shift reviewed the procedure and decided to begin fncreasing RCS pressure.
to a failure of the valve,to properly seat during subsequent  
The shift had noted the 11 caution 11 prior to step 5.43. of 2-0P-1.3 which reads, 11 RCS pressure must remain less than 2000 psig until Step 5.62 is satisfied 11 , and intended to be just below 2000 psig when arriving at step 5.62. However, when the operator closed the accumulator MOV in accordance with step 5.41, he realized that the RCS should have been maintained at less than 1000 psig to perform 2-PT-18.5 (Flushing of Sensitized Stainless Steel Piping -Emergency Borate and Acc~mulator MOV Cycling).
unit operation.  
* It is important to note that it has been our interpretation of Technical Specification 3.3.A.10 that the basis for the requirement (RCS pressure greater than 1000 psig when placing the accumulators in servjce and de-energizing the associated discharge MOVs) was to provide sufficient differential between RCS and accumulator pressures to avoid spurious injections  
2. Inspection  
*. It is from this perspective that no violation of Technical Specifications was initially considered to have occurred as a result of this event. The event investigation focused on the violation of Operating Procedure 2-0P-1.3 when RCS pressure exceeded 1000 psig prior to completion of 2-PT-18.5.
of safety injection  
(3) CORRECTIVE STEPS WHICH 'HAVE BEEN TAKEN AND THE RESULTS ACHIEVED:
check valve 2-SI-91 in accordance  
The accumulator discharge valves were opened and their circuit breakers opened. RCS pressure was controlled per* 2-0P-1.3 and 2-PT-18.5 was
with Engineering  
* performed satisfactorily.
Work -Request 89-6848, dated November 3, 1989, indicated  
The unit SRO and the unit RO were disciplined.
that an incorrect  
gasket had been installed  
during the previous outage. 3. After interim corrective  
action was conducted  
for examples 1 and 2 above on November 1, 1989, incorrect  
gaskets were installed  
in a Unit 2 pressurizer  
safety valve on November 14, 1989, and subsequent  
review revealed potential  
incorrect  
gaskets in the Unit 1 pressurizer  
safety valves. This violation  
has been categorized  
as a Severity Level IV violation  
.(Supplement  
I) for Units 1 and 2. C. * Technical  
Specification  
3.7, Table 3.7.5(a) requires that grab samples be collected  
and analyzed at least once per 12 hours whenever radioactive  
liquid effluent monitoring  
instrumentation  
is out of service. Contrary to the above, grab* samples were not collected  
and analyzed at least once per 12 hours in that, on August 2, 1989, samples for the Component  
cooling service water effluent line were collected  
and analyzed 30 minutes outside the required 12-hour timeframe.  
This violation  
has been categorized  
as a Severity Level IV violation (Supplement  
I) for Units 1 and 2. 2 of 11 ~.;-;-:
* RESPONSE TO NOTICE OF VIOLATION . INSPECTION  
REPORT NOS. 50-280/89-34  
AND 50-281/89-34  
A. 10CFR50, Appendix B, Criterion  
V, requires that activities  
affecting  
quality shall be prescribed  
by documented  
instructions  
or procedures  
appropriate  
to the circumstances  
.. Contrary to the above, activities  
affecting  
quality were not prescribed  
by adequate instructions  
and/or procedures, in that: 1. Operating  
procedure, 2-0P-1.3, Unit Startup Operation  
(350/450 to HSD), Revision dated June 14, 1989, did not adequately  
caution the operators  
to maintain specific pressure control prior to testing reactor coolant system accumulator  
discharge  
valves. On November 21, 1989, during Unit 2 startup, operators  
allowed the reactor coolant system pressure to exceed 1000 psig, prior to opening and de-energizing  
the accumulator  
discharge  
isolation  
valve motor operators, a violation  
of Technical*  
Specification  
3.3.A.10.  
(1) ADMISSION  
OR DENIAL OF THE ALLEGED VIOLATION:  
The violation  
is correct as stated. (2) REASON FOR VIOLATION  
Upon completion  
of OP-7.1.1 (Leak Testing Accumulator  
Check Valves), the electricians  
were directed.to  
reinstall  
the seal-in contacts for the motor operated accumulator  
discharge  
valves. While waiting fof this step to be completed, the operations  
shift reviewed the procedure  
and decided to begin fncreasing  
RCS pressure.  
The shift had noted the 11 caution 11 prior to step 5.43. of 2-0P-1.3 which reads, 11 RCS pressure must remain less than 2000 psig until Step 5.62 is satisfied 11 , and intended to be just below 2000 psig when arriving at step 5.62. However, when the operator closed the accumulator  
MOV in accordance  
with step 5.41, he realized that the RCS should have been maintained  
at less than 1000 psig to perform 2-PT-18.5 (Flushing  
of Sensitized  
Stainless  
Steel Piping -Emergency  
Borate and Acc~mulator  
MOV Cycling).  
* It is important  
to note that it has been our interpretation  
of Technical  
Specification  
3.3.A.10 that the basis for the requirement (RCS pressure greater than 1000 psig when placing the accumulators  
in servjce and de-energizing  
the associated  
discharge  
MOVs) was to provide sufficient  
differential  
between RCS and accumulator  
pressures  
to avoid spurious injections  
*. It is from this perspective  
that no violation  
of Technical  
Specifications  
was initially  
considered  
to have occurred as a result of this event. The event investigation  
focused on the violation  
of Operating  
Procedure  
2-0P-1.3 when RCS pressure exceeded 1000 psig prior to completion  
of 2-PT-18.5.  
(3) CORRECTIVE  
STEPS WHICH 'HAVE BEEN TAKEN AND THE RESULTS ACHIEVED:  
The accumulator  
discharge  
valves were opened and their circuit breakers opened. RCS pressure was controlled  
per* 2-0P-1.3 and 2-PT-18.5  
was * performed  
satisfactorily.  
The unit SRO and the unit RO were disciplined.  
3 of 11 .~--* .. "' ~* *."" *r. *" .. '. ' .   
3 of 11 .~--* .. "' ~* *."" *r. *" .. '. ' .   
** * ,* ' (4) CORRECTIVE  
** * ,* ' (4) CORRECTIVE STEPS WHICH WILL BE TAKEN TO AVOID FURTHER VIOLATIONS:
STEPS WHICH WILL BE TAKEN TO AVOID FURTHER VIOLATIONS:  
The steps in 2-0P-1.3 which are associated with the accumulator check valve test are being evaluated for inclusion in OP-7.1.1.
The steps in 2-0P-1.3 which are associated  
The 11 caution 11 prior to step 5.31 of the existing OP-1.3 which -reads, 11 RCS pressure.
with the accumulator  
must not exceed 1000 psig unti-1 PT-18.5 is complete (Step 5.42). will be strengthened and added to OP-7.1.1.
check valve test are being evaluated  
Technical Specification 3.3.A.10 will be reviewed for potential clarification of both the specification and bases. (5) THE DATE WHEN FULL COMPLIANCE WILL BE ACHIEVED:
for inclusion  
Full compliance will be achieved on June 30, 1990 when the procedures are modified as described above . 4 of 11   
in OP-7.1.1.  
~-A. RESPONSE TO NOTICE OF VIOLATION INSPECTION REPORT NOS. 50-280/89-34 AND 50-281/89-34 10CFR50, Appendix 8, Criterion V, requires that activities affecting quality shall be prescribed by documented instructions or procedures appropriate to the circumstances.
The 11 caution 11 prior to step 5.31 of the existing OP-1.3 which -reads, 11 RCS pressure.  
Contrary to the above, activities affecting quality were not prescribed by adequate instructions and/or procedures, in that: 2. On November 13, 1989, a resin waste transfer evolution was conducted without adequate procedure control resulting in three licensee employees being contaminated when a pipe cap was removed from a pressurized system. (1) ADMISSION OR DENIAL OF THE ALLEGED VIOLATION:
must not exceed 1000 psig unti-1 PT-18.5 is complete (Step 5.42). will be strengthened  
The violation is correct as stated. (2) REASON FOR VIOLATION:
and added to OP-7.1.1.  
The event occurred*
Technical  
due to pressure in a iection of the resin transfer header piping. An inservice leak test was performed on the header line on October 16, 1989. The procedure used is typically performed on piping as part of the Inservice Testing (IST) Program.*
Specification  
Following the use of this procedure~
3.3.A.10 will be reviewed for potential  
the tested piping is returned to service and no instructions are provided for depressurization of the piping. However, the* resin header line was not returned to service and the line could not be drained because decontamination support had not been provided.
clarification  
There was no documentation that the line was left in a pressurized condition, and this information was not provided to the appropriate supervisor.
of both the specification  
In addition, seat leakage on diaphragm valves on the upstream system piping may have contributed to the pressure in the header. On November 13, 1989, while making final hose connections in preparation for transferring resin from the resin waste header to the receiving vessel, it was necessary to remove a cam-lock cap. The cam-lock fitting did not hav~ an upstream isolation valve at the fitting which could be usJd for isolation while the hose connections were being made. The operators began the removal of the cam-lock fitting by opening one of the* dog-ear connectors.*
and bases. (5) THE DATE WHEN FULL COMPLIANCE  
The cap was manipulated in an attempt to relieve any pressure on the 1 i ne. When rio water was observed, .* the remaining*
WILL BE ACHIEVED:  
connector was opened and the cap blew off spraying the employees with contaminated water. The resin transfer procedure did not provide instructions or cautions on the correct operation of the cam-lock fitting. In addition, the procedure did not provide an appropriate level of detail for certain portions of the waste transfer process. * (3) CORRECTIVE STEPS WHICH HAVE BEEN TAKEN AND THE RESULTS ACHIEVED:
Full compliance  
In accordance with station practice, the individuals involved prepared a report of the event and presented it to station management.
will be achieved on June 30, 1990 when the procedures  
are modified as described  
above . 4 of 11   
~-A. RESPONSE TO NOTICE OF VIOLATION  
INSPECTION  
REPORT NOS. 50-280/89-34  
AND 50-281/89-34  
10CFR50, Appendix 8, Criterion  
V, requires that activities  
affecting  
quality shall be prescribed  
by documented  
instructions  
or procedures  
appropriate  
to the circumstances.  
Contrary to the above, activities  
affecting  
quality were not prescribed  
by adequate instructions  
and/or procedures, in that: 2. On November 13, 1989, a resin waste transfer evolution  
was conducted  
without adequate procedure  
control resulting  
in three licensee employees  
being contaminated  
when a pipe cap was removed from a pressurized  
system. (1) ADMISSION  
OR DENIAL OF THE ALLEGED VIOLATION:  
The violation  
is correct as stated. (2) REASON FOR VIOLATION:  
The event occurred*  
due to pressure in a iection of the resin transfer header piping. An inservice  
leak test was performed  
on the header line on October 16, 1989. The procedure  
used is typically  
performed  
on piping as part of the Inservice  
Testing (IST) Program.*  
Following  
the use of this procedure~  
the tested piping is returned to service and no instructions  
are provided for depressurization  
of the piping. However, the* resin header line was not returned to service and the line could not be drained because decontamination  
support had not been provided.  
There was no documentation  
that the line was left in a pressurized  
condition, and this information  
was not provided to the appropriate  
supervisor.  
In addition, seat leakage on diaphragm  
valves on the upstream system piping may have contributed  
to the pressure in the header. On November 13, 1989, while making final hose connections  
in preparation  
for transferring  
resin from the resin waste header to the receiving  
vessel, it was necessary  
to remove a cam-lock cap. The cam-lock fitting did not hav~ an upstream isolation  
valve at the fitting which could be usJd for isolation  
while the hose connections  
were being made. The operators  
began the removal of the cam-lock fitting by opening one of the* dog-ear connectors.*  
The cap was manipulated  
in an attempt to relieve any pressure on the 1 i ne. When rio water was observed, .* the remaining*  
connector  
was opened and the cap blew off spraying the employees  
with contaminated  
water. The resin transfer procedure  
did not provide instructions  
or cautions on the correct operation  
of the cam-lock fitting. In addition, the procedure  
did not provide an appropriate  
level of detail for certain portions of the waste transfer process. * (3) CORRECTIVE  
STEPS WHICH HAVE BEEN TAKEN AND THE RESULTS ACHIEVED:  
In accordance  
with station practice, the individuals  
involved prepared a report of the event and presented  
it to station management.  
5 of 11   
5 of 11   
** * An additional  
**
instruction  
* An additional instruction page for the operation of cam-lock type fittings was developed.
page for the operation  
This attachment will be used with evolutions utilizing cam-lock fittings, until permanent procedure changes can be completed.
of cam-lock type fittings was developed.  
The resin transfer header has been modified to provide an isolation valve upstream at the cam~lock fitting. Resin transfer activities were suspended and no resin transfer activities will occur pending station safety committee (SNSOC) approval of a procedure providing the additional detailed steps for the evolutions involved in the* transfer process. (4) .CORRECTIVE STEPS WHICH WILL BE TAKEN TO AVOID FURTHER VIOLATIONS:
This attachment  
A revision is being made to the procedure for resin transfers to provide more detailed instructions for the evolutions in the resin transfer process including instructions for cam-lock fittings.
will be used with evolutions  
A list of procedures that involve equipment using cam-lock fittings is being developed.
utilizing  
These procedures will be revised to include appropriate cautions.
cam-lock fittings, until permanent  
Since the lack of an appropriate inservice leak testing procedure may have contributed to the event, an additional testing procedure for inser~ice leak testing will be developed to include instructions for d~pressurization of the tested piping if it is not placed in service following the test. (5) THE DATE WHEN FULL COMPLIANCE WILL BE ACHIEVED:
procedure  
Resin transfers may resume when a revised procedure is approved by the SNSOC. The procedure rev1s1ons covering the use of cam-lock fittings and the development of a procedure for inservice leak testing will be completed by June 30, 1990. Full compliance will be achieved on June 30, 1990. -During review of this event and a subsequent event in January involving instrument air to this system, weaknesses were identified in the configuration control and modification turnover processes.
changes can be completed.  
Although not a direct contributor to the above violation, these weaknesses are being reviewed and applicable corrective actions initiated . 6 of 11 i ., "" ,----on" .J   
The resin transfer header has been modified to provide an isolation  
** A. RESPONSE TO NOTICE OF VIOLATION INSPECTION REPORT NOS. 50-280/89-34 AND 50~281/89-34 I0CFR50, Appendix B, Criterion V, requires that activities affecting quality shall be prescribed by documented instructions or procedures appropriate to the circumstances.
valve upstream at the cam~lock fitting. Resin transfer activities  
Contrary to the above, activities affecting quality were not prescribed by adequate instructions and/or procedures, in that: -* 3. On approximately October 25, 1989, the Unit* 2 flood control dikes, which protect against flooding of the service water supply motor control valves to the recirculation spray heat exchangers, were removed with inadequate modification and operation procedure control resulting in heatup of the unit above 350° F, on November 6 and 20, 1989, with inoperable recirculation spray systems, a violation of Technical Specification 3.4. (1) ADMISSION 0~ DENIAL OF THE ALLEGED VIOLATION:
were suspended  
The violation is correct as stated. (2) REASON FOR VIOLATION:
and no resin transfer activities  
A Design Change was being implemented to replace portions of the Service Water piping* and to i_nstall new 8 11 service water supply lines. A portion of the buried piping was routed just north of the service water valve pit containing the service water supply valves. (2-SW-MOV-203A-D) to the recirculation spray heat exchangers.
will occur pending station safety committee (SNSOC) approval of a procedure  
The original design and safety analysis had been prepared anticipating that the missile protection cover plates could be installed without affecting the dikes around the SW valve pit. However, the dikes created an interference when installing the plates, and a Field Change was issued revising the installation drawing to permit temporary removal and replacement of the dike wall 11 as required 11*
providing  
* UFSAR Appendix 9C on the flood control system was not* complete in its description of the flood protection barriers, nor were the dikes physically labeled in the field to identify them as components of the flood _control system. As a result~ the flood protection significance of the dike components was overlooked, and the field change did not provide procedural steps to control this activity nor to limit the period during which the dike wall was removed. (3) CORRECTIVE STEPS WHICH HAVE BEEN TAKEN AND THE RESULTS ACHIEVED: (a) The dikes were reinstalled on the same day the condition was identified. (b) The station flood protection dikes throughout the plant have been labeled with a cautionary
the additional  
_legend. (c) A memorandum describing the incident and taken to ~revent iecurrence of inadequate revi.ew was distributed to Design December 4, 1989. 7 of 11 corrective actions to be Field Change preparation and Engineering personnel on .. .*.** ... ~:**. .........
detailed steps for the evolutions  
_,*~-... -"['"";:",";";-:***
involved in the* transfer process. (4) .CORRECTIVE  
STEPS WHICH WILL BE TAKEN TO AVOID FURTHER VIOLATIONS:  
A revision is being made to the procedure  
for resin transfers  
to provide more detailed instructions  
for the evolutions  
in the resin transfer process including  
instructions  
for cam-lock fittings.  
A list of procedures  
that involve equipment  
using cam-lock fittings is being developed.  
These procedures  
will be revised to include appropriate  
cautions.  
Since the lack of an appropriate  
inservice  
leak testing procedure  
may have contributed  
to the event, an additional  
testing procedure  
for inser~ice  
leak testing will be developed  
to include instructions  
for d~pressurization  
of the tested piping if it is not placed in service following  
the test. (5) THE DATE WHEN FULL COMPLIANCE  
WILL BE ACHIEVED:  
Resin transfers  
may resume when a revised procedure  
is approved by the SNSOC. The procedure  
rev1s1ons  
covering the use of cam-lock fittings and the development  
of a procedure  
for inservice  
leak testing will be completed  
by June 30, 1990. Full compliance  
will be achieved on June 30, 1990. -During review of this event and a subsequent  
event in January involving  
instrument  
air to this system, weaknesses  
were identified  
in the configuration  
control and modification  
turnover processes.  
Although not a direct contributor  
to the above violation, these weaknesses  
are being reviewed and applicable  
corrective  
actions initiated . 6 of 11 i ., "" ,----on" .J   
** A. RESPONSE TO NOTICE OF VIOLATION  
INSPECTION  
REPORT NOS. 50-280/89-34  
AND 50~281/89-34  
I0CFR50, Appendix B, Criterion  
V, requires that activities  
affecting  
quality shall be prescribed  
by documented  
instructions  
or procedures  
appropriate  
to the circumstances.  
Contrary to the above, activities  
affecting  
quality were not prescribed  
by adequate instructions  
and/or procedures, in that: -* 3. On approximately  
October 25, 1989, the Unit* 2 flood control dikes, which protect against flooding of the service water supply motor control valves to the recirculation  
spray heat exchangers, were removed with inadequate  
modification  
and operation  
procedure  
control resulting  
in heatup of the unit above 350° F, on November 6 and 20, 1989, with inoperable  
recirculation  
spray systems, a violation  
of Technical  
Specification  
3.4. (1) ADMISSION  
0~ DENIAL OF THE ALLEGED VIOLATION:  
The violation  
is correct as stated. (2) REASON FOR VIOLATION:  
A Design Change was being implemented  
to replace portions of the Service Water piping* and to i_nstall new 8 11 service water supply lines. A portion of the buried piping was routed just north of the service water valve pit containing  
the service water supply valves. (2-SW-MOV-203A-D)  
to the recirculation  
spray heat exchangers.  
The original design and safety analysis had been prepared anticipating  
that the missile protection  
cover plates could be installed  
without affecting  
the dikes around the SW valve pit. However, the dikes created an interference  
when installing  
the plates, and a Field Change was issued revising the installation  
drawing to permit temporary  
removal and replacement  
of the dike wall 11 as required 11* * UFSAR Appendix 9C on the flood control system was not* complete in its description  
of the flood protection  
barriers, nor were the dikes physically  
labeled in the field to identify them as components  
of the flood _control system. As a result~ the flood protection  
significance  
of the dike components  
was overlooked, and the field change did not provide procedural  
steps to control this activity nor to limit the period during which the dike wall was removed. (3) CORRECTIVE  
STEPS WHICH HAVE BEEN TAKEN AND THE RESULTS ACHIEVED: (a) The dikes were reinstalled  
on the same day the condition  
was identified. (b) The station flood protection  
dikes throughout  
the plant have been labeled with a cautionary  
_legend. (c) A memorandum  
describing  
the incident and taken to ~revent iecurrence  
of inadequate  
revi.ew was distributed  
to Design December 4, 1989. 7 of 11 corrective  
actions to be Field Change preparation  
and Engineering  
personnel  
on .. .*.** ... ~:**. .........  
_,*~-... -"['"";:",";";-:***
I I -I I I -------------
I I -I I I -------------
* * (4) CORRECTIVE  
* * (4) CORRECTIVE STEPS WHICH WILL BE TAKEN TO AVOID FURTHER VIOLATIONS:
STEPS WHICH WILL BE TAKEN TO AVOID FURTHER VIOLATIONS:  
The following corrective actions will be taken to avoid recurrence: (a) Information on the flood protection barriers will be included in the continuing training sessions for the Technical_
The following  
Support Staff to enhance general awareness of the need to maintain integrity of these barriers. (b) The UFSAR section on flood control will be reviewed and a change request processed to provide more complete information on the flood protection barriers. (c) An engineering review of the adequacy of testing and maintenance of flood control measures has *been initiated. ( 5) THE .DATE WHEN FULL COMPLIANCE WILL BE ACHIEVED:
corrective  
Full compliance will be achieved when the corrective actions identified in item (4) above are completed on September 30, 1990. The UFSAR change wfll be included in the annual update subsequent to September 30, 1990. 8 of 11   
actions will be taken to avoid recurrence: (a) Information  
*** B. RESPONSE TO NOTICE OF VIOLATION INSPECTION REPORT NOS. 50-280/89-34 AND 50-281/89-34 10 CFR 50, Appendix B, Criterion VIII, requires that measures.and controls . shall be established to prevent the use of incorrect or defective material, parts,* and components.
on the flood protection  
Contrary to the above, adequate measures were not established to .Prevent incorrect gaskets from being installed in components in that: 1. Work Order 87218, dated October 28, 1989, identified that an incorrect gasket had been installed in safety injection check valve 2-Sl-79 during the previous outage. This condition had contributed to a failure of the valve to properly seat during subsequent unit operation.
barriers will be included in the continuing  
: 2. Inspection of safety injection check valve 2-SI..;.91 in accordance with
training sessions for the Technical_  
* Engineering Work Request 89-684B, dated November 3, 1989, indicated that an incorrect gasket had been installed during the previous outage. 3. After interim corrective action was conducted for examples 1 and 2 above on November 1, 1989, incorrect gaskets were installed in a Unit 2 pressurizer safety valve on November 14, 1989, and subsequent review revealed potential incorrect gaskets in the Unit 1 pressurizer safety valves. (1) ADMISSION OR DENIAL OF THE ALLEGED VIOLATION:
Support Staff to enhance general awareness  
The violation is correct as stated. (2) REASON FOR VIOLATION:
of the need to maintain integrity  
Inaccuracies existed in certain aspects of model work orders in the area of parts and associated stock numbers required to perform the task. The model work orders were not subject to a formal control program and verification of the parts listed on the model work order were not performed by planning or maintenance personnel.
of these barriers. (b) The UFSAR section on flood control will be reviewed and a change request processed  
This omission resulted in incorrect gaskets being installed in two (2) safety injection check valves (2-SI-79/2-SI-91) when model work order parts listings were used. Another incident occurred whereby wrong gasket material was installed on a Unit 2 pressurizer safety valve due to the same inadequacie~.  
to provide more complete information  
* (3) CORRECTIVE STEPS WHICH HAVE BEEN TAKEN AND THE RESULTS ACHIEVED:
on the flood protection  
Upon initi,ll discovery of wrong material installation on certain safety related* components, an investigation was performed within the maintenance department.
barriers. (c) An engineering  
The problem was determined to be inadequate parts verification prior to .job implementation.
review of the adequacy of testing and maintenance  
The information concerning parts listed on the model work order was being incorrectly assumed as being correct. Once this problem was identified, an interim verification of parts for safety related work was established.
of flood control measures has *been initiated. ( 5) THE .DATE WHEN FULL COMPLIANCE  
The corrective steps taken by the Maintenance Department were as follows: a. Oeve l opment of an "Engineering Parts Validation Program" which established the process whereby engineering personnel ensure that 9 of 11   
WILL BE ACHIEVED:  
~. b. correct parts/components (with regard to technical data and materials) are installed in the respective system per design and licensing requirements.
Full compliance  
This program applies to safety related and non-safety related * (with special regulatory significance) work orders. Implementation of this 11 Validation Program 11 was effective on November 1, 1989. The Maintenance Engineering Department currently performs this function.
will be achieved when the corrective  
Since _the implementation of the parts validation process, there was the one instance referenced in the violation where the Maintenance Department inadvertently installed wrong gaskets in a Unit 2 pressurizer safety valve. At that time,. the validation process was still in the initial stages, and it is felt that the incident was an isolated case. The validation process of parts verification now is very closely controlled.
actions identified  
Since the incorrect gasket installation on November 14, 1989, there have been no identified cases of incorrect parts usage. (4) CORRECTIVE STEPS WHICH WILL BE TAKEN TO AVOID FURTHER VIOLATIONS:
in item (4) above are completed  
Concerning the Unit 1 Pressurizer Safety Valves and the possibility of incorrect gasket material being installed, the safety significance of this configuration has been evaluated and determined to be acceptable for continued operation.
on September  
Work requests will be submitted to remove valves and inspect/replace gaskets as necessary to ensure the c-orrect gasket type is installed.
30, 1990. The UFSAR change wfll be included in the annual update subsequent  
This replacement of gaskets will be performed at the next refueling outage. (5) THE DATE WHEN FULL COMPLIANCE WILL BE ACHIEVED:
to September  
Full compliance with regard to programmatic changes for parts validation measures was achieved on November 15, 1989, although the pressurizer safety
30, 1990. 8 of 11   
* valve gasket concern on Unit 1 will be resolved during the upcoming refueling outage. 10 of 11   
*** B. RESPONSE TO NOTICE OF VIOLATION  
.. ' RESPONSE TO NOTICE OF VIOLATION INSPECTION REPORT NOS. 50-280/89-34 AND 50-281/89-34 C. Technical Specification 3.7 5 Table 3.7.5(a) requires that grab samples be collected and analyzed at least once per 12 hours whenever radioactive liquid effluent monitoring instrumentation is out of service. Contrary to the aboves grab samples were not collected and analyzed at least once per 12 hours in thats on August 2, 1989 5
INSPECTION  
* samples for the component cooling service water effluent line were collected and analyzed 30 minutes outside the required 12-hour time frame. (1) ADMISSION OR DENIAL OF THE ALLEGED VIOLATION:
REPORT NOS. 50-280/89-34  
The violation is correct ~s stated. (2) REASON FOR VIOLATION:
AND 50-281/89-34  
The cause of the event was personnel error. The turbine building operator log requires sampling once per eight hour shift. The previous sample had been obtained early in the shift, and the liquid waste control room operator did not effectively communicate to the turbine building operator when the next sample would be required .. (3) CORRECTIVE STEPS WHICH HAVE BEEN TAKEN AND THE RESULTS ACHIEVED:
10 CFR 50, Appendix B, Criterion  
The event was reviewed with the turbine building and liquid waste operators.
VIII, requires that measures.and  
controls . shall be established  
to prevent the use of incorrect  
or defective  
material, parts,* and components.  
Contrary to the above, adequate measures were not established  
to .Prevent incorrect  
gaskets from being installed  
in components  
in that: 1. Work Order 87218, dated October 28, 1989, identified  
that an incorrect  
gasket had been installed  
in safety injection  
check valve 2-Sl-79 during the previous outage. This condition  
had contributed  
to a failure of the valve to properly seat during subsequent  
unit operation.  
2. Inspection  
of safety injection  
check valve 2-SI..;.91  
in accordance  
with * Engineering  
Work Request 89-684B, dated November 3, 1989, indicated  
that an incorrect  
gasket had been installed  
during the previous outage. 3. After interim corrective  
action was conducted  
for examples 1 and 2 above on November 1, 1989, incorrect  
gaskets were installed  
in a Unit 2 pressurizer  
safety valve on November 14, 1989, and subsequent  
review revealed potential  
incorrect  
gaskets in the Unit 1 pressurizer  
safety valves. (1) ADMISSION  
OR DENIAL OF THE ALLEGED VIOLATION:  
The violation  
is correct as stated. (2) REASON FOR VIOLATION:  
Inaccuracies  
existed in certain aspects of model work orders in the area of parts and associated  
stock numbers required to perform the task. The model work orders were not subject to a formal control program and verification  
of the parts listed on the model work order were not performed  
by planning or maintenance  
personnel.  
This omission resulted in incorrect  
gaskets being installed  
in two (2) safety injection  
check valves (2-SI-79/2-SI-91)  
when model work order parts listings were used. Another incident occurred whereby wrong gasket material was installed  
on a Unit 2 pressurizer  
safety valve due to the same inadequacie~.  
* (3) CORRECTIVE  
STEPS WHICH HAVE BEEN TAKEN AND THE RESULTS ACHIEVED:  
Upon initi,ll discovery  
of wrong material installation  
on certain safety related* components, an investigation  
was performed  
within the maintenance  
department.  
The problem was determined  
to be inadequate  
parts verification  
prior to .job implementation.  
The information  
concerning  
parts listed on the model work order was being incorrectly  
assumed as being correct. Once this problem was identified, an interim verification  
of parts for safety related work was established.  
The corrective  
steps taken by the Maintenance  
Department  
were as follows: a. Oeve l opment of an "Engineering  
Parts Validation  
Program" which established  
the process whereby engineering  
personnel  
ensure that 9 of 11   
~. b. correct parts/components (with regard to technical  
data and materials)  
are installed  
in the respective  
system per design and licensing  
requirements.  
This program applies to safety related and non-safety  
related * (with special regulatory  
significance)  
work orders. Implementation  
of this 11 Validation  
Program 11 was effective  
on November 1, 1989. The Maintenance  
Engineering  
Department  
currently  
performs this function.  
Since _the implementation  
of the parts validation  
process, there was the one instance referenced  
in the violation  
where the Maintenance  
Department  
inadvertently  
installed  
wrong gaskets in a Unit 2 pressurizer  
safety valve. At that time,. the validation  
process was still in the initial stages, and it is felt that the incident was an isolated case. The validation  
process of parts verification  
now is very closely controlled.  
Since the incorrect  
gasket installation  
on November 14, 1989, there have been no identified  
cases of incorrect  
parts usage. (4) CORRECTIVE  
STEPS WHICH WILL BE TAKEN TO AVOID FURTHER VIOLATIONS:  
Concerning  
the Unit 1 Pressurizer  
Safety Valves and the possibility  
of incorrect  
gasket material being installed, the safety significance  
of this configuration  
has been evaluated  
and determined  
to be acceptable  
for continued  
operation.  
Work requests will be submitted  
to remove valves and inspect/replace  
gaskets as necessary  
to ensure the c-orrect gasket type is installed.  
This replacement  
of gaskets will be performed  
at the next refueling  
outage. (5) THE DATE WHEN FULL COMPLIANCE  
WILL BE ACHIEVED:  
Full compliance  
with regard to programmatic  
changes for parts validation  
measures was achieved on November 15, 1989, although the pressurizer  
safety * valve gasket concern on Unit 1 will be resolved during the upcoming refueling  
outage. 10 of 11   
.. ' RESPONSE TO NOTICE OF VIOLATION  
INSPECTION  
REPORT NOS. 50-280/89-34  
AND 50-281/89-34  
C. Technical  
Specification  
3.7 5 Table 3.7.5(a) requires that grab samples be collected  
and analyzed at least once per 12 hours whenever radioactive  
liquid effluent monitoring  
instrumentation  
is out of service. Contrary to the aboves grab samples were not collected  
and analyzed at least once per 12 hours in thats on August 2, 1989 5 * samples for the component  
cooling service water effluent line were collected  
and analyzed 30 minutes outside the required 12-hour time frame. (1) ADMISSION  
OR DENIAL OF THE ALLEGED VIOLATION:  
The violation  
is correct ~s stated. (2) REASON FOR VIOLATION:  
The cause of the event was personnel  
error. The turbine building operator log requires sampling once per eight hour shift. The previous sample had been obtained early in the shift, and the liquid waste control room operator did not effectively  
communicate  
to the turbine building operator when the next sample would be required .. (3) CORRECTIVE  
STEPS WHICH HAVE BEEN TAKEN AND THE RESULTS ACHIEVED:  
The event was reviewed with the turbine building and liquid waste operators.  
The liquid waste operator was disciplined.  
The liquid waste operator was disciplined.  
* * The liquid waste control room operator's  
*
log has been revised to include a section that specifically  
* The liquid waste control room operator's log has been revised to include a section that specifically identifies the time and date the heat exchangers were last sampled and the ti~e when the next sample is to be taken. (4) CORRECTIVE STEPS WHICH WILL BE TAKEN TO AVOID FURTHER VIOLATIONS:
identifies  
Design work is in progress to replace the existi~g component cooling service water radiation monitoring system concurrent with replatement of the Component Cooling Water Heat Exchangers.
the time and date the heat exchangers  
The new design consists of a detector that will be mounted in a dry well in each heat exchanger.
were last sampled and the ti~e when the next sample is to be taken. (4) CORRECTIVE  
This design contains no piping subject to fouling and provides an individual detector for each heat exchanger.
STEPS WHICH WILL BE TAKEN TO AVOID FURTHER VIOLATIONS:  
(5) THE DATE WHEN FULL COMPLIANCE WILL BE ACHIEVED:
Design work is in progress to replace the existi~g component  
Ful.l compliance with Technical Specifications was achieved August 2, 1989. The heat exchanger replacement project is underway and is currently scheduled to be completed by Spring, 1991. 11 of 11}}
cooling service water radiation  
monitoring  
system concurrent  
with replatement  
of the Component  
Cooling Water Heat Exchangers.  
The new design consists of a detector that will be mounted in a dry well in each heat exchanger.  
This design contains no piping subject to fouling and provides an individual  
detector for each heat exchanger.  
(5) THE DATE WHEN FULL COMPLIANCE  
WILL BE ACHIEVED:  
Ful.l compliance  
with Technical  
Specifications  
was achieved August 2, 1989. The heat exchanger  
replacement  
project is underway and is currently  
scheduled  
to be completed  
by Spring, 1991. 11 of 11
}}

Revision as of 15:06, 31 July 2019

Responds to NRC 891222 Ltr Re Violations Noted in Insp Repts 50-280/89-34 & 50-281/89-34 on 891029-1125.Corrective Actions:Steps in Operating Procedure 2-OP-1.3 Associated W/ Valve Test Being Evaluated for Inclusion in OP-7.1.1
ML18152A488
Person / Time
Site: Surry  Dominion icon.png
Issue date: 02/06/1990
From: Stewart W
VIRGINIA POWER (VIRGINIA ELECTRIC & POWER CO.)
To:
NRC OFFICE OF INFORMATION RESOURCES MANAGEMENT (IRM)
References
89-880, NUDOCS 9002220547
Download: ML18152A488 (13)


Text

-. VIRGINIA ELECTRIC AND POWER COMPANY RICHMOND, VIRGINIA 23261 February 6, 1990 United States Nuclear Regulatory Commission Attention:

Document Control Desk Washington, D.C. 20555 Gentlemen:

VIRGINIA ELECTRIC AND POWER COMPANY SORRY POWER STATION UNITS 1 AND 2 REPLY TO A NOTICE OF VIOLATION

-Ser_i al No. NL/RPC Docket Nos. License Nos. NRC INSPECTION REPORT NOS. 50-280/89-34 AND 50-281/89-34 89-880 R3 50-280 50-281 . DPR-32 DPR-37 We have reviewed your letter dated December 22, 1989, in reference to the NRC inspection conducted-on October 29 -November 25, 1989, for Surry Power Station. The inspection was reported in Inspection Report Nos! 50-280/89-34 and 50-281/89-34.

Our response to the violations described in the Notice of Violation is provided in Attachment

1. Your letter expressed concern over the material condition of the process monitoring instrumentation.

You requested that we address our program to assure that process monitoring equipment is maintained operable and outline specific actions being taken to return inoperable process instrumentation to service in an expeditious manner.* -Operability of the process monitoring instrumentation is demonstrated periodically through the station's surveillance and testing program. If a component is found to be inoperable, alternative measures are employed to monitor the parameter in accordance with Technical Specifications and a.station deviation is submitted.

On December 21, 1989, a station deviation trending report was submitted to the Chairman of the Station Nuclear Safety Operating Committee (SNSOC), which discussed recurring problems with process radiation monitors.

To more fully address these issues, the SNSOC established a subcommittee composed of senior technical staff members. The subcommittee has been tasked to review process radiation monitoring operations data sources, including equipment operability history, and to submit a report on its findings by February 28, 1990. 6ased on this report, SNSOC will assign further actions as appropriate.

We are keeping the NRC Resident Inspectors informed of the progress and results of this review. The project to replace and return _the component cooling water (CCW) heat exchanger service water effluent monitors to operation is being implemented in conjunction with the ongoing project to replace the CCW heat exchangers.

One. of the four installed heat exchangers has been replaced and the installation of the associated service water effluent monitor is scheduled for completion in February 1990, subject to receipt of the remaining equipment.

The next two CCW heat exchangers are scheduled for replacement during the Unit I ref~jPel~;/

9002220547 900206 PDR ADOCK 05000280 I,., Q PNV The final CCW heat The alternative remain in effect outage currently planned for the fourth quarter of 1990. exchanger is scheduled for the second quarter of 1991. sampling measures specified by Technical Specifications will until completion of the project. In a telephone conversation between Mr. S. Shaeffer of the NRC Region II staff and Mr. D. Sommers of my staff, an extension of 15 days was granted for our reply to this Notice of Violation.

We have no objection to this inspection report being made a matter of public disclosure.

Should you have .any further questions, please contact us. Very truly yours, &\-S~ W. L. Stewart Senior Vice President

-Nuclear Attachment cc: U.S. Nuclear Regulatory Commission Region II 101 Marietta Street, N.W. Suite 2900 , Atlanta, Georgia 30323 Mr. W. E. Holland NRC Senior Resident Inspector Surry Power Station --------, I NRC Comment ATTACHMENT 1 REPLY TO A NOTICE OF VIOLATION REPORTED DORING THE NRC INSPECTIONS ON OCTOBER 29 -NOVtMBER 25, 1989 INSPECTION REPORT NOS. 50-280/89-34 AND 50-281/89-34 During the Nuclear Regulatory Commission (NRC) inspection conducted on October 29 -November 25, 1989, violations of NRC requirements were identified.

In accordance with the '.'General Statement of Policy and Procedure for NRC Enforcement Actions, 11 10 CFR Part 2, Appendix C ( 1989), the violations are listed below:

  • A. 10 CFR 50, Appendix B, Criteriori V, requires that activities affecting quality shall be prescribed by documented instructions or procedures appropriate to the circumstances.

Contrary to the above, activities affecting quality were not prescribed by adequate instructions and/or procedures, in that: 1. Operating Procedure, 2-0P-1.3, Unit Startup Operation (350/450 to HSD), Revision dated June 14, 1989, did not adequately caution the operators to maintain specific pressure control prior to testing reactor coolant system accumulator discharge valves. On November 21, 1989, during Unit 2 startu~, operators allowed the reactor coolant system pressure to eiceed 1000 psig, prior to cipening and de-energizing the accumulator discharge isolation valve motor operators, a violation of Technical . Specification 3.3.A.10.

2. On November 13, 1989, a resin waste transfer evolution was conducted without adequate*

procedure control resulting in three licensee employees being contaminated when a pipe cap was removed from a pressurized system; 3. On approximately October 25, 1989, the Unit 2 flood control dikes, which protect against flooding of the service water supply motor control valves to the recirculation spray heat exchangers, were removed with inadequate modification and operation procedure control resulttng in heatup of the unit above 350°F, on November 6 and 20, 1989, with inoperable recirculation spray systems, a violation of Technical Specification 3.4. This violation has been. categorized as a Severity Level IV violation (Supplement I) for Unit 2. B. 10 CFR 50, Appendix B, Criterion VII, requires that measures and controls shall be established to prevent the use of incorrect or defective material, parts, and components.

1 of 11

  • Contrary to . the above, adequate measures were not established to prevent incorrect gaskets from being installed in components in that: 1. Work Order 87218, dated October 28, 1989, identified that an incorrect gasket had been installed in. safety injection check valve 2""'.SI-79 during the previous outage. This condition had contributed to a failure of the valve,to properly seat during subsequent unit operation.
2. Inspection of safety injection check valve 2-SI-91 in accordance with Engineering Work -Request 89-6848, dated November 3, 1989, indicated that an incorrect gasket had been installed during the previous outage. 3. After interim corrective action was conducted for examples 1 and 2 above on November 1, 1989, incorrect gaskets were installed in a Unit 2 pressurizer safety valve on November 14, 1989, and subsequent review revealed potential incorrect gaskets in the Unit 1 pressurizer safety valves. This violation has been categorized as a Severity Level IV violation

.(Supplement I) for Units 1 and 2. C.

  • Technical Specification 3.7, Table 3.7.5(a) requires that grab samples be collected and analyzed at least once per 12 hours1.388889e-4 days <br />0.00333 hours <br />1.984127e-5 weeks <br />4.566e-6 months <br /> whenever radioactive liquid effluent monitoring instrumentation is out of service. Contrary to the above, grab* samples were not collected and analyzed at least once per 12 hours1.388889e-4 days <br />0.00333 hours <br />1.984127e-5 weeks <br />4.566e-6 months <br /> in that, on August 2, 1989, samples for the Component cooling service water effluent line were collected and analyzed 30 minutes outside the required 12-hour timeframe.

This violation has been categorized as a Severity Level IV violation (Supplement I) for Units 1 and 2. 2 of 11 ~.;-;-:

  • RESPONSE TO NOTICE OF VIOLATION . INSPECTION REPORT NOS. 50-280/89-34 AND 50-281/89-34 A. 10CFR50, Appendix B, Criterion V, requires that activities affecting quality shall be prescribed by documented instructions or procedures appropriate to the circumstances

.. Contrary to the above, activities affecting quality were not prescribed by adequate instructions and/or procedures, in that: 1. Operating procedure, 2-0P-1.3, Unit Startup Operation (350/450 to HSD), Revision dated June 14, 1989, did not adequately caution the operators to maintain specific pressure control prior to testing reactor coolant system accumulator discharge valves. On November 21, 1989, during Unit 2 startup, operators allowed the reactor coolant system pressure to exceed 1000 psig, prior to opening and de-energizing the accumulator discharge isolation valve motor operators, a violation of Technical*

Specification 3.3.A.10.

(1) ADMISSION OR DENIAL OF THE ALLEGED VIOLATION:

The violation is correct as stated. (2) REASON FOR VIOLATION Upon completion of OP-7.1.1 (Leak Testing Accumulator Check Valves), the electricians were directed.to reinstall the seal-in contacts for the motor operated accumulator discharge valves. While waiting fof this step to be completed, the operations shift reviewed the procedure and decided to begin fncreasing RCS pressure.

The shift had noted the 11 caution 11 prior to step 5.43. of 2-0P-1.3 which reads, 11 RCS pressure must remain less than 2000 psig until Step 5.62 is satisfied 11 , and intended to be just below 2000 psig when arriving at step 5.62. However, when the operator closed the accumulator MOV in accordance with step 5.41, he realized that the RCS should have been maintained at less than 1000 psig to perform 2-PT-18.5 (Flushing of Sensitized Stainless Steel Piping -Emergency Borate and Acc~mulator MOV Cycling).

  • It is important to note that it has been our interpretation of Technical Specification 3.3.A.10 that the basis for the requirement (RCS pressure greater than 1000 psig when placing the accumulators in servjce and de-energizing the associated discharge MOVs) was to provide sufficient differential between RCS and accumulator pressures to avoid spurious injections
  • . It is from this perspective that no violation of Technical Specifications was initially considered to have occurred as a result of this event. The event investigation focused on the violation of Operating Procedure 2-0P-1.3 when RCS pressure exceeded 1000 psig prior to completion of 2-PT-18.5.

(3) CORRECTIVE STEPS WHICH 'HAVE BEEN TAKEN AND THE RESULTS ACHIEVED:

The accumulator discharge valves were opened and their circuit breakers opened. RCS pressure was controlled per* 2-0P-1.3 and 2-PT-18.5 was

  • performed satisfactorily.

The unit SRO and the unit RO were disciplined.

3 of 11 .~--* .. "' ~* *."" *r. *" .. '. ' .

    • * ,* ' (4) CORRECTIVE STEPS WHICH WILL BE TAKEN TO AVOID FURTHER VIOLATIONS:

The steps in 2-0P-1.3 which are associated with the accumulator check valve test are being evaluated for inclusion in OP-7.1.1.

The 11 caution 11 prior to step 5.31 of the existing OP-1.3 which -reads, 11 RCS pressure.

must not exceed 1000 psig unti-1 PT-18.5 is complete (Step 5.42). will be strengthened and added to OP-7.1.1.

Technical Specification 3.3.A.10 will be reviewed for potential clarification of both the specification and bases. (5) THE DATE WHEN FULL COMPLIANCE WILL BE ACHIEVED:

Full compliance will be achieved on June 30, 1990 when the procedures are modified as described above . 4 of 11

~-A. RESPONSE TO NOTICE OF VIOLATION INSPECTION REPORT NOS. 50-280/89-34 AND 50-281/89-34 10CFR50, Appendix 8, Criterion V, requires that activities affecting quality shall be prescribed by documented instructions or procedures appropriate to the circumstances.

Contrary to the above, activities affecting quality were not prescribed by adequate instructions and/or procedures, in that: 2. On November 13, 1989, a resin waste transfer evolution was conducted without adequate procedure control resulting in three licensee employees being contaminated when a pipe cap was removed from a pressurized system. (1) ADMISSION OR DENIAL OF THE ALLEGED VIOLATION:

The violation is correct as stated. (2) REASON FOR VIOLATION:

The event occurred*

due to pressure in a iection of the resin transfer header piping. An inservice leak test was performed on the header line on October 16, 1989. The procedure used is typically performed on piping as part of the Inservice Testing (IST) Program.*

Following the use of this procedure~

the tested piping is returned to service and no instructions are provided for depressurization of the piping. However, the* resin header line was not returned to service and the line could not be drained because decontamination support had not been provided.

There was no documentation that the line was left in a pressurized condition, and this information was not provided to the appropriate supervisor.

In addition, seat leakage on diaphragm valves on the upstream system piping may have contributed to the pressure in the header. On November 13, 1989, while making final hose connections in preparation for transferring resin from the resin waste header to the receiving vessel, it was necessary to remove a cam-lock cap. The cam-lock fitting did not hav~ an upstream isolation valve at the fitting which could be usJd for isolation while the hose connections were being made. The operators began the removal of the cam-lock fitting by opening one of the* dog-ear connectors.*

The cap was manipulated in an attempt to relieve any pressure on the 1 i ne. When rio water was observed, .* the remaining*

connector was opened and the cap blew off spraying the employees with contaminated water. The resin transfer procedure did not provide instructions or cautions on the correct operation of the cam-lock fitting. In addition, the procedure did not provide an appropriate level of detail for certain portions of the waste transfer process. * (3) CORRECTIVE STEPS WHICH HAVE BEEN TAKEN AND THE RESULTS ACHIEVED:

In accordance with station practice, the individuals involved prepared a report of the event and presented it to station management.

5 of 11

  • An additional instruction page for the operation of cam-lock type fittings was developed.

This attachment will be used with evolutions utilizing cam-lock fittings, until permanent procedure changes can be completed.

The resin transfer header has been modified to provide an isolation valve upstream at the cam~lock fitting. Resin transfer activities were suspended and no resin transfer activities will occur pending station safety committee (SNSOC) approval of a procedure providing the additional detailed steps for the evolutions involved in the* transfer process. (4) .CORRECTIVE STEPS WHICH WILL BE TAKEN TO AVOID FURTHER VIOLATIONS:

A revision is being made to the procedure for resin transfers to provide more detailed instructions for the evolutions in the resin transfer process including instructions for cam-lock fittings.

A list of procedures that involve equipment using cam-lock fittings is being developed.

These procedures will be revised to include appropriate cautions.

Since the lack of an appropriate inservice leak testing procedure may have contributed to the event, an additional testing procedure for inser~ice leak testing will be developed to include instructions for d~pressurization of the tested piping if it is not placed in service following the test. (5) THE DATE WHEN FULL COMPLIANCE WILL BE ACHIEVED:

Resin transfers may resume when a revised procedure is approved by the SNSOC. The procedure rev1s1ons covering the use of cam-lock fittings and the development of a procedure for inservice leak testing will be completed by June 30, 1990. Full compliance will be achieved on June 30, 1990. -During review of this event and a subsequent event in January involving instrument air to this system, weaknesses were identified in the configuration control and modification turnover processes.

Although not a direct contributor to the above violation, these weaknesses are being reviewed and applicable corrective actions initiated . 6 of 11 i ., "" ,----on" .J

    • A. RESPONSE TO NOTICE OF VIOLATION INSPECTION REPORT NOS. 50-280/89-34 AND 50~281/89-34 I0CFR50, Appendix B, Criterion V, requires that activities affecting quality shall be prescribed by documented instructions or procedures appropriate to the circumstances.

Contrary to the above, activities affecting quality were not prescribed by adequate instructions and/or procedures, in that: -* 3. On approximately October 25, 1989, the Unit* 2 flood control dikes, which protect against flooding of the service water supply motor control valves to the recirculation spray heat exchangers, were removed with inadequate modification and operation procedure control resulting in heatup of the unit above 350° F, on November 6 and 20, 1989, with inoperable recirculation spray systems, a violation of Technical Specification 3.4. (1) ADMISSION 0~ DENIAL OF THE ALLEGED VIOLATION:

The violation is correct as stated. (2) REASON FOR VIOLATION:

A Design Change was being implemented to replace portions of the Service Water piping* and to i_nstall new 8 11 service water supply lines. A portion of the buried piping was routed just north of the service water valve pit containing the service water supply valves. (2-SW-MOV-203A-D) to the recirculation spray heat exchangers.

The original design and safety analysis had been prepared anticipating that the missile protection cover plates could be installed without affecting the dikes around the SW valve pit. However, the dikes created an interference when installing the plates, and a Field Change was issued revising the installation drawing to permit temporary removal and replacement of the dike wall 11 as required 11*

  • UFSAR Appendix 9C on the flood control system was not* complete in its description of the flood protection barriers, nor were the dikes physically labeled in the field to identify them as components of the flood _control system. As a result~ the flood protection significance of the dike components was overlooked, and the field change did not provide procedural steps to control this activity nor to limit the period during which the dike wall was removed. (3) CORRECTIVE STEPS WHICH HAVE BEEN TAKEN AND THE RESULTS ACHIEVED: (a) The dikes were reinstalled on the same day the condition was identified. (b) The station flood protection dikes throughout the plant have been labeled with a cautionary

_legend. (c) A memorandum describing the incident and taken to ~revent iecurrence of inadequate revi.ew was distributed to Design December 4, 1989. 7 of 11 corrective actions to be Field Change preparation and Engineering personnel on .. .*.** ... ~:**. .........

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I I -I I I -------------

  • * (4) CORRECTIVE STEPS WHICH WILL BE TAKEN TO AVOID FURTHER VIOLATIONS:

The following corrective actions will be taken to avoid recurrence: (a) Information on the flood protection barriers will be included in the continuing training sessions for the Technical_

Support Staff to enhance general awareness of the need to maintain integrity of these barriers. (b) The UFSAR section on flood control will be reviewed and a change request processed to provide more complete information on the flood protection barriers. (c) An engineering review of the adequacy of testing and maintenance of flood control measures has *been initiated. ( 5) THE .DATE WHEN FULL COMPLIANCE WILL BE ACHIEVED:

Full compliance will be achieved when the corrective actions identified in item (4) above are completed on September 30, 1990. The UFSAR change wfll be included in the annual update subsequent to September 30, 1990. 8 of 11

Contrary to the above, adequate measures were not established to .Prevent incorrect gaskets from being installed in components in that: 1. Work Order 87218, dated October 28, 1989, identified that an incorrect gasket had been installed in safety injection check valve 2-Sl-79 during the previous outage. This condition had contributed to a failure of the valve to properly seat during subsequent unit operation.

2. Inspection of safety injection check valve 2-SI..;.91 in accordance with
  • Engineering Work Request 89-684B, dated November 3, 1989, indicated that an incorrect gasket had been installed during the previous outage. 3. After interim corrective action was conducted for examples 1 and 2 above on November 1, 1989, incorrect gaskets were installed in a Unit 2 pressurizer safety valve on November 14, 1989, and subsequent review revealed potential incorrect gaskets in the Unit 1 pressurizer safety valves. (1) ADMISSION OR DENIAL OF THE ALLEGED VIOLATION:

The violation is correct as stated. (2) REASON FOR VIOLATION:

Inaccuracies existed in certain aspects of model work orders in the area of parts and associated stock numbers required to perform the task. The model work orders were not subject to a formal control program and verification of the parts listed on the model work order were not performed by planning or maintenance personnel.

This omission resulted in incorrect gaskets being installed in two (2) safety injection check valves (2-SI-79/2-SI-91) when model work order parts listings were used. Another incident occurred whereby wrong gasket material was installed on a Unit 2 pressurizer safety valve due to the same inadequacie~.

  • (3) CORRECTIVE STEPS WHICH HAVE BEEN TAKEN AND THE RESULTS ACHIEVED:

Upon initi,ll discovery of wrong material installation on certain safety related* components, an investigation was performed within the maintenance department.

The problem was determined to be inadequate parts verification prior to .job implementation.

The information concerning parts listed on the model work order was being incorrectly assumed as being correct. Once this problem was identified, an interim verification of parts for safety related work was established.

The corrective steps taken by the Maintenance Department were as follows: a. Oeve l opment of an "Engineering Parts Validation Program" which established the process whereby engineering personnel ensure that 9 of 11

~. b. correct parts/components (with regard to technical data and materials) are installed in the respective system per design and licensing requirements.

This program applies to safety related and non-safety related * (with special regulatory significance) work orders. Implementation of this 11 Validation Program 11 was effective on November 1, 1989. The Maintenance Engineering Department currently performs this function.

Since _the implementation of the parts validation process, there was the one instance referenced in the violation where the Maintenance Department inadvertently installed wrong gaskets in a Unit 2 pressurizer safety valve. At that time,. the validation process was still in the initial stages, and it is felt that the incident was an isolated case. The validation process of parts verification now is very closely controlled.

Since the incorrect gasket installation on November 14, 1989, there have been no identified cases of incorrect parts usage. (4) CORRECTIVE STEPS WHICH WILL BE TAKEN TO AVOID FURTHER VIOLATIONS:

Concerning the Unit 1 Pressurizer Safety Valves and the possibility of incorrect gasket material being installed, the safety significance of this configuration has been evaluated and determined to be acceptable for continued operation.

Work requests will be submitted to remove valves and inspect/replace gaskets as necessary to ensure the c-orrect gasket type is installed.

This replacement of gaskets will be performed at the next refueling outage. (5) THE DATE WHEN FULL COMPLIANCE WILL BE ACHIEVED:

Full compliance with regard to programmatic changes for parts validation measures was achieved on November 15, 1989, although the pressurizer safety

  • valve gasket concern on Unit 1 will be resolved during the upcoming refueling outage. 10 of 11

.. ' RESPONSE TO NOTICE OF VIOLATION INSPECTION REPORT NOS. 50-280/89-34 AND 50-281/89-34 C. Technical Specification 3.7 5 Table 3.7.5(a) requires that grab samples be collected and analyzed at least once per 12 hours1.388889e-4 days <br />0.00333 hours <br />1.984127e-5 weeks <br />4.566e-6 months <br /> whenever radioactive liquid effluent monitoring instrumentation is out of service. Contrary to the aboves grab samples were not collected and analyzed at least once per 12 hours1.388889e-4 days <br />0.00333 hours <br />1.984127e-5 weeks <br />4.566e-6 months <br /> in thats on August 2, 1989 5

  • samples for the component cooling service water effluent line were collected and analyzed 30 minutes outside the required 12-hour time frame. (1) ADMISSION OR DENIAL OF THE ALLEGED VIOLATION:

The violation is correct ~s stated. (2) REASON FOR VIOLATION:

The cause of the event was personnel error. The turbine building operator log requires sampling once per eight hour shift. The previous sample had been obtained early in the shift, and the liquid waste control room operator did not effectively communicate to the turbine building operator when the next sample would be required .. (3) CORRECTIVE STEPS WHICH HAVE BEEN TAKEN AND THE RESULTS ACHIEVED:

The event was reviewed with the turbine building and liquid waste operators.

The liquid waste operator was disciplined.

  • The liquid waste control room operator's log has been revised to include a section that specifically identifies the time and date the heat exchangers were last sampled and the ti~e when the next sample is to be taken. (4) CORRECTIVE STEPS WHICH WILL BE TAKEN TO AVOID FURTHER VIOLATIONS:

Design work is in progress to replace the existi~g component cooling service water radiation monitoring system concurrent with replatement of the Component Cooling Water Heat Exchangers.

The new design consists of a detector that will be mounted in a dry well in each heat exchanger.

This design contains no piping subject to fouling and provides an individual detector for each heat exchanger.

(5) THE DATE WHEN FULL COMPLIANCE WILL BE ACHIEVED:

Ful.l compliance with Technical Specifications was achieved August 2, 1989. The heat exchanger replacement project is underway and is currently scheduled to be completed by Spring, 1991. 11 of 11