IR 05000275/2006003: Difference between revisions

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| issue date = 08/14/2006
| issue date = 08/14/2006
| title = IR 05000275-06-003, 05000323-06-003; 4/1/06 - 6/30/06; Diablo Canyon Power Plant Units 1 and 2; Inservice Inspection Activities, Operability Evaluations, Refueling and Outage Activities, and Access Control to Radiologically Significant Area
| title = IR 05000275-06-003, 05000323-06-003; 4/1/06 - 6/30/06; Diablo Canyon Power Plant Units 1 and 2; Inservice Inspection Activities, Operability Evaluations, Refueling and Outage Activities, and Access Control to Radiologically Significant Area
| author name = Jones W B
| author name = Jones W
| author affiliation = NRC/RGN-IV/DRP/RPB-B
| author affiliation = NRC/RGN-IV/DRP/RPB-B
| addressee name = Keenan J S
| addressee name = Keenan J
| addressee affiliation = Pacific Gas & Electric Co
| addressee affiliation = Pacific Gas & Electric Co
| docket = 05000275, 05000323
| docket = 05000275, 05000323
Line 18: Line 18:


=Text=
=Text=
{{#Wiki_filter:
{{#Wiki_filter:August 14, 2006 John Senior Vice President - Generation
[[Issue date::August 14, 2006]]
 
John Senior Vice President - Generation


and Chief Nuclear Officer
and Chief Nuclear Officer
Line 31: Line 28:
Mail Code B32
Mail Code B32


San Francisco, CA 94177-0001
San Francisco, CA 94177-0001SUBJECT:DIABLO CANYON POWER PLANT - NRC INTEGRATED INSPECTION REPORT 05000275/2006003 AND 05000323/2006003
 
SUBJECT: DIABLO CANYON POWER PLANT - NRC INTEGRATED INSPECTION REPORT 05000275/2006003 AND 05000323/2006003


==Dear Mr. Keenan:==
==Dear Mr. Keenan:==
Line 69: Line 64:
In accordance with 10 CFR 2.390 of the NRC's "Rules of Practice," a copy of this letter and its enclosure will be available electronically for public inspection in the NRC Public Document
In accordance with 10 CFR 2.390 of the NRC's "Rules of Practice," a copy of this letter and its enclosure will be available electronically for public inspection in the NRC Public Document


Room or from the Publicly Available Records (PARS) component of NRC's document system (ADAMS). ADAMS is accessible from the NRC Web site at http://www.nrc.gov/reading-
Room or from the Publicly Available Records (PARS) component of NRC's document system (ADAMS). ADAMS is accessible from the NRC Web site at http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room).
rm/adams.html (the Public Electronic Reading Room).


Sincerely,/RA/William B. Jones, Chief Project Branch B
Sincerely,
/RA/William B. Jones, Chief Project Branch B


Division of Reactor Projects Dockets: 50-275 50-323
Division of Reactor Projects Dockets: 50-275 50-323
Line 85: Line 80:
and 05000323/2006003
and 05000323/2006003


===w/attachment:===
w/attachment: Supplemental Information
Supplemental Information cc w/enclosure:
Donna Jacobs


Vice President, Nuclear Services
REGION IVDockets:50-275, 50-323 Licenses:DPR-80, DPR-82 Report:05000275/2006003 05000323/2006003Licensee:Pacific Gas and Electric Company (PG&E)
Facility:Diablo Canyon Power Plant, Units 1 and 2 Location:7 1/2 miles NW of Avila Beach Avila Beach, CaliforniaDates:April 1 through June 30, 2006 Inspectors:T. Jackson, Senior Resident Inspector T. McConnell, Resident Inspector


Diablo Canyon Power Plant
S. Graves, Reactor Inspector


P.O. Box 56
P. Gage, Senior Operations Engineer


Avila Beach, CA 93424 James R. Becker, Vice President Diablo Canyon Operations and
R. Lantz, Senior Emergency Preparedness Inspector


Station Director, Pacific Gas and
J. Tapia, Senior Reactor Inspector


Electric Company
B. Tharakan, Health PhysicistApproved By:W. B. Jones, Chief, Project Branch B Division of Reactor Projects Enclosure-2-


Diablo Canyon Power Plant
=SUMMARY OF FINDINGS=
IR 05000275/2006-003, 05000323/2006-003; 4/1/06 - 6/30/06; Diablo Canyon Power Plant


P.O. Box 56
Units 1 and 2; Inservice Inspection Activities, Operability Evaluations, Refueling and Outage


Avila Beach, CA 93424 Sierra Club San Lucia Chapter ATTN: Andrew Christie
Activities, and Access Control to Radiologically Significant Areas.


P.O. Box 15755
This report covered a 13-week period of inspection by resident inspectors and announced inspections in radiation protection, emergency preparedness, operator requalification, and in-


San Luis Obispo, CA 93406 Pacific Gas and Electric Company- 3 -
service inspections. One self-revealing and four NRC-identified, Green, noncited violations were identified. The significance of most findings is indicated by their color (Green, White,
Nancy Culver San Luis Obispo Mothers for Peace
Yellow, or Red) using Inspection Manual Chapter 0609, "Significance Determination Process."


P.O. Box 164
Findings for which the Significance Determination Process does not apply may be Green or be assigned a severity level after NRC management review. The NRC's program for overseeing the safe operation of commercial nuclear power reactors is described in NUREG-1649, "Reactor


Pismo Beach, CA 93448 Chairman San Luis Obispo County Board of
Oversight Process," Revision 3, dated July 2000.A.


Supervisors
===NRC-Identified and Self-Revealing Findings===


County Government Building
===Cornerstone: Mitigating Systems===
: '''Green.'''
A self-revealing, noncited violation of 10 CFR Part 50, Appendix B,Criterion XVI, was determined for the failure of operations personnel to promptly identify a condition adverse to quality. Specifically, on November 27, 2005, operators failed to document, in the corrective action program, an unexpected level drop in Accumulator 1-3. Failure to enter the occurrence into the corrective action program precluded actions that would have addressed similar conditions that resulted in a subsequent event involving an unexpected level drop and water hammer associated with Accumulator 2-3, which occurred on May 21, 2006.


1055 Monterey Street, Suite D430
This issue was entered into Pacific Gas and Electric Company's corrective action program as Action Request A0669468.


San Luis Obispo, CA 93408 Truman Burns\Robert Kinosian California Public Utilities Commission
The finding is greater than minor because it is associated with the Mitigating Systems Cornerstone attribute of configuration control and affects the associated cornerstone objective to ensure the availability, reliability, and capability of systems that respond to initiating events to prevent undesirable consequences.


505 Van Ness Ave., Rm. 4102
Using the Inspection Manual Chapter 0609, "Significance Determination


San Francisco, CA 94102-3298 Diablo Canyon Independent Safety Committee Robert R. Wellington, Esq.
Process," Phase 1 Worksheet, the finding is determined to be of very low safety significance because the finding did not represent a loss of a safety function, an actual loss of a safety-related train for greater than its Technical Specification allowed outage time, or screen as potentially risk-significant due to seismic, fire, flooding, or severe weather initiating events. The finding had a crosscutting aspect in the area of problem identification and resolution because operations personnel failed to promptly identify, in the corrective action program, the unexpected level drop in Accumulator 1-3 (Section 1R15).*Green. An NRC-identified, noncited violation of Technical Specification 5.4.1.a for an inadequate procedure, Procedure OP A-2:II, "Reactor Vessel - Draining the RCS to the Vessel Flange - With Fuel in Vessel," Revision 33A. Specifically, on April 20, 2006, while operators depressurized the reactor coolant system, with Enclosure-4-water level 2 feet below the reactor vessel flange, the two required level instruments, wide-range reactor vessel refueling level indication system and


Legal Counsel
LI-400, read 15 inches higher than actual reactor vessel water level. The inspectors determined that the procedure was not adequate because prior operating experience had not been incorporated into the procedure that demonstrated the level instruments would read nonconservatively during the reactor coolant system depressurization. Also, Procedure OP A-2:II did not have criteria that alerted operators to abnormal level instrument deviations that may be caused by phenomenon outside of the level deviations expected by the reactor coolant system depressurization. Pacific Gas and Electric Company has planned to evaluate potential changes to Procedure OP A-2:II and reactor coolant system water level instrumentation when used during reactor coolant system depressurization. This issue was entered into Pacific Gas and Electric


857 Cass Street, Suite D
Company's corrective action program as Action Requests A0664484, A0672419, and A0672422.


Monterey, CA 93940 Director, Radiological Health Branch State Department of Health Services
The finding is greater than minor because it is associated with the Mitigating Systems Cornerstone attribute of procedure quality and affects the associated cornerstone objective to ensure the availability, reliability, and capability of systems that respond to initiating events to prevent undesirable consequences.


P.O. Box 997414 (MS 7610)
Using Inspection Manual Chapter 0609, Appendix G, Attachment 1, Checklist 3, the finding is determined to be of very low safety significance since an optional set of instrumentation provided accurate reactor coolant system level indication and there was no loss of reactor coolant system inventory control. The finding had a crosscutting aspect in the area of human performance for resources because Pacific Gas and Electric Company failed to ensure the adequacy of procedures used for reactor vessel level monitoring to ensure nuclear safety (Section 1R20).*Green. An NRC-identified noncited violation of 10 CFR Part 50, Criterion XVI,"Corrective Actions," was determined for the failure to prevent recurrence of a similar failures, that occurred between 2003 and 2006, of Limitorque SMB-000 actuators in the auxiliary feedwater sy stem. Pacific Gas and Electric Company staff failed to adequately troubleshoot and provide for timely corrective actions regarding auxiliary feedwater control valves that failed due to high actuator torque switch resistance. This finding was entered into Pacific Gas and Electric


Sacramento, CA 95899-7414 Richard F. Locke, Esq.
Company's corrective action program as Nonconformance Report N0002205.


Pacific Gas and Electric Company
The finding is greater than minor because it is associated with the Mitigating Systems Cornerstone attribute of equipment performance and affects the associated cornerstone objective to ensure the availability, reliability, and capability of systems that respond to initiating events to prevent undesirable consequences. Using the Inspection Manual Chapter 0609, "Significance


P.O. Box 7442
Determination Process," Phase 1 Worksheet, the finding is determined to be of very low safety significance because it did not represent an actual loss of safety function, represent an actual loss of safety function for a single train for greater than the Technical Specification allowed outage time, or screen as potentially risk significant due to seismic, fire, flooding, or severe weather initiating events. The finding had a crosscutting aspect in the area of problem identification and Enclosure-5-resolution since Pacific Gas and Electric Company staff failed to adequately trend, assess, and troubleshoot previous Limitorque SMB-000 actuator failures (Section 4OA5.3).


San Francisco, CA 94120 City Editor The Tribune
===Cornerstone: Barrier Integrity===
: '''Green.'''
An NRC-identified noncited violation of Technical Specification 5.4.1 was identified because Pacific Gas and Electric Company failed to follow the procedure for ensuring that welding preheat temperatures were verified prior to welding. Specifically, during the replacement of Component Cooling Water


3825 South Higuera Street
Valves 279 and 280, which provide cooling to the reactor vessel support pads,
Pacific Gas and Electric Company failed to verify that the minimum welding preheat temperature of 50°F was met, and could not demonstrate that the ambient temperature was greater than 50°F. Pacific Gas and Electric Company surveyed the area and entered the finding into their corrective action program as


P.O. Box 112
Action Request A0665588.


San Luis Obispo, CA 93406-0112 James D. Boyd, Commissioner California Energy Commission
The finding was greater than minor because it was associated with the human performance attribute of the Barrier Integrity Cornerstone and impacted the cornerstone objective of providing reasonable assurance that physical design barriers, in this case the reactor coolant system, protect the public from radio-


1516 Ninth Street (MS 34)
nuclide releases caused by accidents or events. The finding was determined to be of very low safety significance based on management review of the plant conditions at the time the performance deficiency occurred (defueled) and the condition was evaluated prior to the plant entering Mode 5 (Section 1R08).


Sacramento, CA 95814 Pacific Gas and Electric Company- 4 -
===Cornerstone: Occupational Radiation Safety===
Jennifer Tang Field Representative
: '''Green.'''
The inspectors identified a noncited violation of 10 CFR 20.1501(a)because Pacific Gas and Electric Company failed to survey to determine the extent and magnitude of radiation levels and evaluate the radiological hazards.


United States Senator Barbara Boxer
Specifically, on April 18, 2006, the inspectors identified elevated radiation levels near two chemical volume control system valves located in a hallway on the 100-foot elevation of Unit 2. Pacific Gas and Electric Company confirmed elevated radiation levels near the valves were as high as 200 millirem per hour on contact and 28 millirem per hour at 30 centimeters. Pacific Gas and Electric


1700 Montgomery Street, Suite 240
Company surveyed the area and entered the finding into their corrective action program as Action Request 0665039.


San Francisco, CA 94111 Chief, Radiological Emergency Preparedness Section
The finding was greater than minor because it was associated with the Occupational Radiation Safety Cornerstone attribute of Exposure Control and


Oakland Field Office
Monitoring and affected the cornerstone objective to ensure the adequate protection of a worker's health and safety from exposure to radiation because workers could have unknowingly received additional radiation exposure. When going through the Occupational Radiation Safety Significance Determination


Chemical and Nuclear Preparedness
Process, the finding was determined to be of very low safety significance because it was not an as low as is reasonably achievable finding. There was no overexposure or substantial potential for an overexposure, and the ability to assess dose was not compromised. The finding also had crosscutting aspects Enclosure-6-associated with human performance because adequate resources were not established for the survey requirements (Section 2OS1).


and Protection Division
Enclosure-7-


Department of Homeland Security
=REPORT DETAILS=


1111 Broadway, Suite 1200
===Summary of Plant Status===


Oakland, CA 94607-4052 Enclosure Electronic distribution by RIV:
Diablo Canyon Unit 1 operated at 100 percent power for this inspection period.
Regional Administrator (BSM1)DRP Director (ATH)DRS Director (DDC)DRS Deputy Director (RJC1)Senior Resident Inspector (TWJ)Branch Chief, DRP/B (WBJ)Senior Project Engineer, DRP/E (FLB2)Team Leader, DRP/TSS (RLN1)RITS Coordinator (KEG)DRS STA (DAP)V. Dricks, PAO (VLD)J. Lamb, OEDO RIV Coordinator (JGL1)ROPreports DC Site Secretary (AWC1)W. A. Maier, RSLO (WAM)SUNSI Review Completed: __wbj___ADAMS: Yes G No Initials: __wbj_ Publicly Available G Non-Publicly Available G Sensitive Non-SensitiveR:\_REACTORS\_DC\2006\DC2006-03RP-TWJ.wpdML062270051RIV:RI:DRP/BSRIDRS/EB1DRS/EB2DRS/OB TAMcConnellTWJacksonJAClarkLJSmithATGody E - WBJones T - WBJones /RA/ /RA/ /RA/8/11/068/1/068/3/068/1/068/2/06DRS/PSBC:DRP/BMPShannonWBJones /RA/ /RA/8/3/068/14/06OFFICIAL RECORD COPY T=Telephone E=E-mail F=Fax U.S. NUCLEAR REGULATORY COMMISSION Enclosure-1-REGION IVDockets:50-275, 50-323 Licenses:DPR-80, DPR-82 Report:05000275/2006003 05000323/2006003Licensee:Pacific Gas and Electric Company (PG&E)
Facility:Diablo Canyon Power Plant, Units 1 and 2 Location:7 1/2 miles NW of Avila Beach Avila Beach, CaliforniaDates:April 1 through June 30, 2006 Inspectors:T. Jackson, Senior Resident Inspector T. McConnell, Resident Inspector


S. Graves, Reactor Inspector
Diablo Canyon Unit 2 began this inspection period at 100 percent power and entered Refueling Outage 2R13 on April 17, 2006. Unit 2 entered Mode 6 (Refueling) for core offload operations


P. Gage, Senior Operations Engineer
on April 20, which was completed on April 25. Unit 2 entered Mode 6 on May 11 when


R. Lantz, Senior Emergency Preparedness Inspector
operators began reloading fuel into the core, and then entered Mode 5 (Cold Shutdown) on


J. Tapia, Senior Reactor Inspector
May 17 when maintenance personnel tensioned the reactor vessel head. Operators


B. Tharakan, Health PhysicistApproved By:W. B. Jones, Chief, Project Branch B Division of Reactor Projects Enclosure-2-
commenced a heatup of the reactor coolant system (RCS), and Unit 2 entered Mode 4 (Hot


=SUMMARY OF FINDINGS=
Shutdown) on May 21 and Mode 3 (Hot Standby) on May 23. On May 24, operators proceeded
IR 05000275/2006-003, 05000323/2006-003; 4/1/06 - 6/30/06; Diablo Canyon Power Plant


Units 1 and 2; Inservice Inspection Activities, Operability Evaluations, Refueling and Outage
with reactor startup, entering Mode 2 (Startup). Operators increased reactor power, and Unit 2


Activities, and Access Control to Radiologically Significant Areas.
entered Mode 1 (Power Operations) on May 25. On May 25, Unit 2 was paralleled to the grid, ending Refueling Outage 2R13. On May 26, the operators removed the unit from the grid due


This report covered a 13-week period of inspection by resident inspectors and announced inspections in radiation protection, emergency preparedness, operator requalification, and in-
to a seal rub on the low pressure turbine. The main turbine was subsequently paralleled to the


service inspections. One self-revealing and four NRC-identified, Green, noncited violations were identified. The significance of most findings is indicated by their color (Green, White,
grid on the same day. Operators continued to raise reactor power and, on June 5, Unit 2
Yellow, or Red) using Inspection Manual Chapter 0609, "Significance Determination Process."


Findings for which the Significance Determination Process does not apply may be Green or be assigned a severity level after NRC management review. The NRC's program for overseeing the safe operation of commercial nuclear power reactors is described in NUREG-1649, "Reactor
reached 100 percent power. On June 21, Unit 2 reduced power to 82 percent to perform


Oversight Process," Revision 3, dated July 2000.A.
maintenance on high pressure turbine governor Valve FCV-142. Unit 2 was returned to


===NRC-Identified and Self-Revealing Findings===
100 percent power on the same day and remained at that power level for the remainder of the


===Cornerstone: Mitigating Systems===
inspection period.1.REACTOR SAFETY Cornerstones: Initiating Events, Mitigating Systems, and Barrier Integrity1R04Equipment Alignments (71111.04)
: '''Green.'''
A self-revealing, noncited violation of 10 CFR Part 50, Appendix B,Criterion XVI, was determined for the failure of operations personnel to promptly identify a condition adverse to quality. Specifically, on November 27, 2005, operators failed to document, in the corrective action program, an unexpected level drop in Accumulator 1-3. Failure to enter the occurrence into the corrective action program precluded actions that would have addressed similar conditions that resulted in a subsequent event involving an unexpected level drop and water hammer associated with Accumulator 2-3, which occurred on May 21, 2006.


This issue was entered into Pacific Gas and Electric Company's corrective action program as Action Request A0669468.
===.1 Partial System Walkdowns===


The finding is greater than minor because it is associated with the Mitigating Systems Cornerstone attribute of configuration control and affects the associated cornerstone objective to ensure the availability, reliability, and capability of systems that respond to initiating events to prevent undesirable consequences.
====a. Inspection Scope====
The inspectors:
: (1) walked down portions of the three below listed risk-important systems and reviewed plant procedures and document s to verify that critical portions of the selected systems were correctly aligned; and
: (2) compared deficiencies identified


Using the Inspection Manual Chapter 0609, "Significance Determination
during the walkdown to the Final Safety Analysis Report (FSAR) Update and corrective


Process," Phase 1 Worksheet, the finding is determined to be of very low safety significance because the finding did not represent a loss of a safety function, an actual loss of a safety-related train for greater than its Technical Specification allowed outage time, or screen as potentially risk-significant due to seismic, fire, flooding, or severe weather initiating events. The finding had a crosscutting aspect in the area of problem identification and resolution because operations personnel failed to promptly identify, in the corrective action program, the unexpected level drop in Accumulator 1-3 (Section 1R15).*Green. An NRC-identified, noncited violation of Technical Specification 5.4.1.a for an inadequate procedure, Procedure OP A-2:II, "Reactor Vessel - Draining the RCS to the Vessel Flange - With Fuel in Vessel," Revision 33A. Specifically, on April 20, 2006, while operators depressurized the reactor coolant system, with Enclosure-4-water level 2 feet below the reactor vessel flange, the two required level instruments, wide-range reactor vessel refueling level indication system and
action program (CAP) to ensure problems were being identified and corrected.*April 17, 2006:  Unit 2, RCS piping*May 5, 2006:  Unit 2, Vital Batteries 2-1, 2-2, and 2-3
*June 28, 2006:  Unit 1, Safety Injection Pump 1-1 Documents reviewed by the inspectors included:
*Procedure OP B-3A:II, "Safety Injection System Alignment Verification for Plant Startup," Revision 23,*Drawing 106709, "Safety Injection," Sheet 4, Revision 54
-8-The inspectors completed three samples.


LI-400, read 15 inches higher than actual reactor vessel water level. The inspectors determined that the procedure was not adequate because prior operating experience had not been incorporated into the procedure that demonstrated the level instruments would read nonconservatively during the reactor coolant system depressurization. Also, Procedure OP A-2:II did not have criteria that alerted operators to abnormal level instrument deviations that may be caused by phenomenon outside of the level deviations expected by the reactor coolant system depressurization. Pacific Gas and Electric Company has planned to evaluate potential changes to Procedure OP A-2:II and reactor coolant system water level instrumentation when used during reactor coolant system depressurization. This issue was entered into Pacific Gas and Electric
====b. Findings====
No findings of significance were identified.


Company's corrective action program as Action Requests A0664484, A0672419, and A0672422.
===.2 Complete System Walkdown===


The finding is greater than minor because it is associated with the Mitigating Systems Cornerstone attribute of procedure quality and affects the associated cornerstone objective to ensure the availability, reliability, and capability of systems that respond to initiating events to prevent undesirable consequences.
====a. Inspection Scope====
The inspectors:
: (1) reviewed plant procedures, calculations, the FSAR Update, Technical Specifications (TSs), and vendor manuals to determine the impact of ultra-low


Using Inspection Manual Chapter 0609, Appendix G, Attachment 1, Checklist 3, the finding is determined to be of very low safety significance since an optional set of instrumentation provided accurate reactor coolant system level indication and there was no loss of reactor coolant system inventory control. The finding had a crosscutting aspect in the area of human performance for resources because Pacific Gas and Electric Company failed to ensure the adequacy of procedures used for reactor vessel level monitoring to ensure nuclear safety (Section 1R20).*Green. An NRC-identified noncited violation of 10 CFR Part 50, Criterion XVI,"Corrective Actions," was determined for the failure to prevent recurrence of a similar failures, that occurred between 2003 and 2006, of Limitorque SMB-000 actuators in the auxiliary feedwater sy stem. Pacific Gas and Electric Company staff failed to adequately troubleshoot and provide for timely corrective actions regarding auxiliary feedwater control valves that failed due to high actuator torque switch resistance. This finding was entered into Pacific Gas and Electric
sulfur diesel fuel on the capability of the diesel engine generators;
: (2) reviewed


Company's corrective action program as Nonconformance Report N0002205.
outstanding design issues, operator workarounds, and FSAR Update documents to


The finding is greater than minor because it is associated with the Mitigating Systems Cornerstone attribute of equipment performance and affects the associated cornerstone objective to ensure the availability, reliability, and capability of systems that respond to initiating events to prevent undesirable consequences. Using the Inspection Manual Chapter 0609, "Significance
determine if open issues affected the functionality of the diesel engine generators; and
: (3) verified that Pacific Gas and Electric Company (PG&E) was identifying and resolving


Determination Process," Phase 1 Worksheet, the finding is determined to be of very low safety significance because it did not represent an actual loss of safety function, represent an actual loss of safety function for a single train for greater than the Technical Specification allowed outage time, or screen as potentially risk significant due to seismic, fire, flooding, or severe weather initiating events. The finding had a crosscutting aspect in the area of problem identification and Enclosure-5-resolution since Pacific Gas and Electric Company staff failed to adequately trend, assess, and troubleshoot previous Limitorque SMB-000 actuator failures (Section 4OA5.3).
equipment alignment problems. Documents revi ewed by the inspectors are listed in the attachment.


===Cornerstone: Barrier Integrity===
The inspectors completed one sample.
: '''Green.'''
An NRC-identified noncited violation of Technical Specification 5.4.1 was identified because Pacific Gas and Electric Company failed to follow the procedure for ensuring that welding preheat temperatures were verified prior to welding. Specifically, during the replacement of Component Cooling Water


Valves 279 and 280, which provide cooling to the reactor vessel support pads,
====b. Findings====
Pacific Gas and Electric Company failed to verify that the minimum welding preheat temperature of 50°F was met, and could not demonstrate that the ambient temperature was greater than 50°F. Pacific Gas and Electric Company surveyed the area and entered the finding into their corrective action program as
No findings of significance were identified.
{{a|1R05}}
==1R05 Fire Protection (71111.05)==


Action Request A0665588.
===.1 Quarterly Inspection===


The finding was greater than minor because it was associated with the human performance attribute of the Barrier Integrity Cornerstone and impacted the cornerstone objective of providing reasonable assurance that physical design barriers, in this case the reactor coolant system, protect the public from radio-
====a. Inspection Scope====
The inspectors walked down the six below listed plant areas to assess the material condition of active and passive fire protection features and their operational lineup and


nuclide releases caused by accidents or events. The finding was determined to be of very low safety significance based on management review of the plant conditions at the time the performance deficiency occurred (defueled) and the condition was evaluated prior to the plant entering Mode 5 (Section 1R08).
readiness. The inspectors:
: (1) verified that transient combustibles and hot work


===Cornerstone: Occupational Radiation Safety===
activities were controlled in accordance with plant procedures;
: '''Green.'''
: (2) observed the
The inspectors identified a noncited violation of 10 CFR 20.1501(a)because Pacific Gas and Electric Company failed to survey to determine the extent and magnitude of radiation levels and evaluate the radiological hazards.


Specifically, on April 18, 2006, the inspectors identified elevated radiation levels near two chemical volume control system valves located in a hallway on the 100-foot elevation of Unit 2. Pacific Gas and Electric Company confirmed elevated radiation levels near the valves were as high as 200 millirem per hour on contact and 28 millirem per hour at 30 centimeters. Pacific Gas and Electric
condition of fire detection devices to verify they remained functional;
: (3) observed fire


Company surveyed the area and entered the finding into their corrective action program as Action Request 0665039.
suppression systems to verify they re mained functional and that access to manual actuators was unobstructed;
: (4) verified that fire extinguishers and hose stations were


The finding was greater than minor because it was associated with the Occupational Radiation Safety Cornerstone attribute of Exposure Control and
provided at their designated locations and that they were in a satisfactory condition;
: (5) verified that passive fire protection features (electrical raceway barriers, fire doors, fire dampers, steel fire proofing, penetration seals, and oil collection systems) were in a


Monitoring and affected the cornerstone objective to ensure the adequate protection of a worker's health and safety from exposure to radiation because workers could have unknowingly received additional radiation exposure. When going through the Occupational Radiation Safety Significance Determination
satisfactory material condition;
: (6) verified that adequate compensatory measures were


Process, the finding was determined to be of very low safety significance because it was not an as low as is reasonably achievable finding. There was no overexposure or substantial potential for an overexposure, and the ability to assess dose was not compromised. The finding also had crosscutting aspects Enclosure-6-associated with human performance because adequate resources were not established for the survey requirements (Section 2OS1).
established for degraded or inoperable fire protection features and that the


Enclosure-7-
compensatory measures were commensurate with the significance of the deficiency; and
: (7) reviewed the FSAR Update to determine if PG&E identified and corrected fire


=REPORT DETAILS=
protection problems.*April 10, 2006:  Unit 2, 140 foot turbine building
-9-*April 14, 2006:  Unit 2, 64 foot auxiliary building*May 1, 2006:  Units 1 and 2, intake structure
*May 2, 2006:  Unit 2, Containment Fire Zones 1A, 1B, and 1C
*May 2, 2006:  Unit 1, 85 foot auxiliary building
*May 8, 2006: Security diesel engine generator building Documents reviewed by the inspectors are listed in the attachment.


===Summary of Plant Status===
The inspectors completed six samples.


Diablo Canyon Unit 1 operated at 100 percent power for this inspection period.
====b. Findings====
No findings of significance were identified.
{{a|1R06}}
==1R06 Flood Protection Measures (71111.06)==


Diablo Canyon Unit 2 began this inspection period at 100 percent power and entered Refueling Outage 2R13 on April 17, 2006. Unit 2 entered Mode 6 (Refueling) for core offload operations
Annual External Flooding


on April 20, which was completed on April 25. Unit 2 entered Mode 6 on May 11 when
====a. Inspection Scope====
The inspectors:
: (1) reviewed the FSAR Update, the flooding analysis, and plant procedures to assess seasonal susceptibilities involving external flooding;
: (2) reviewed


operators began reloading fuel into the core, and then entered Mode 5 (Cold Shutdown) on
the FSAR Update and CAP to determine if PG&E identified and corrected flooding


May 17 when maintenance personnel tensioned the reactor vessel head. Operators
problems;
: (3) inspected underground bunkers/manholes to verify the adequacy of:
: (a) sump pumps,
: (b) level alarm circuits,
: (c) cable splices subject to submergence, and
: (d) drainage for bunkers/manholes;
: (4) verified that operator actions for coping with


commenced a heatup of the reactor coolant system (RCS), and Unit 2 entered Mode 4 (Hot
flooding can reasonably achieve the desired outcomes; and
: (5) walked down the one


Shutdown) on May 21 and Mode 3 (Hot Standby) on May 23. On May 24, operators proceeded
below listed area to verify the adequacy of:
: (a) equipment seals located below the


with reactor startup, entering Mode 2 (Startup). Operators increased reactor power, and Unit 2
floodline,
: (b) floor and wall penetration seals,
: (c) watertight door seals,
: (d) common drain


entered Mode 1 (Power Operations) on May 25. On May 25, Unit 2 was paralleled to the grid, ending Refueling Outage 2R13. On May 26, the operators removed the unit from the grid due
lines and sumps,
: (e) sump pumps, level alarms, and control circuits, and
: (f) temporary or


to a seal rub on the low pressure turbine. The main turbine was subsequently paralleled to the
removable flood barriers.*April 2, 2006:  Units 1 and 2, 500 kV switchyard Pullboxes W-3 and W-4


grid on the same day. Operators continued to raise reactor power and, on June 5, Unit 2
Documents reviewed by the inspectors are listed in the attachment.


reached 100 percent power. On June 21, Unit 2 reduced power to 82 percent to perform
The inspectors completed one sample.


maintenance on high pressure turbine governor Valve FCV-142. Unit 2 was returned to
====b. Findings====
No findings of significance were identified.
{{a|1R07}}
==1R07 Heat Sink Performance (71111.07)==


100 percent power on the same day and remained at that power level for the remainder of the
====a. Inspection Scope====
The inspectors reviewed PG&E's programs, verified performance against industry standards, and reviewed critical operating parameters and maintenance records for


inspection period.1.REACTOR SAFETY Cornerstones: Initiating Events, Mitigating Systems, and Barrier Integrity1R04Equipment Alignments (71111.04)
Component Cooling Water Heat Exchangers 1-1 and 1-2. The inspectors verified that:  
-10-(1) performance tests were satisfactorily conducted for heat exchangers/heat sinks and reviewed for problems or errors;
: (2) PG&E utilized the periodic maintenance method


===.1 Partial System Walkdowns===
outlined in Electric Power Research Institute NP-7552, "Heat Exchanger Performance


====a. Inspection Scope====
Monitoring Guidelines;"
The inspectors:
: (3) PG&E properly utilized biofouling controls;
: (1) walked down portions of the three below listed risk-important systems and reviewed plant procedures and document s to verify that critical portions of the selected systems were correctly aligned; and
: (4) PG&E's heat
: (2) compared deficiencies identified


during the walkdown to the Final Safety Analysis Report (FSAR) Update and corrective
exchanger inspections adequately assessed the state of cleanliness of their tubes, and
: (5) the heat exchanger was correctly categorized under the Maintenance Rule.


action program (CAP) to ensure problems were being identified and corrected.*April 17, 2006:  Unit 2, RCS piping*May 5, 2006:  Unit 2, Vital Batteries 2-1, 2-2, and 2-3
Documents reviewed by the inspectors included Procedure PEP -234, "CCW Heat Exchanger Performance Test," Revision 9.
*June 28, 2006:  Unit 1, Safety Injection Pump 1-1 Documents reviewed by the inspectors included:
 
*Procedure OP B-3A:II, "Safety Injection System Alignment Verification for Plant Startup," Revision 23,*Drawing 106709, "Safety Injection," Sheet 4, Revision 54
The inspectors completed one sample.
-8-The inspectors completed three samples.


====b. Findings====
====b. Findings====
No findings of significance were identified.
No findings of significance were identified.
{{a|1R08}}
==1R08 Inservice Inspection Activities (71111.08)==
===.1 Inspection Activities Other Than Steam Generator Tube Inspections, Pressurized Water===


===.2 Complete System Walkdown===
Reactor Vessel Upper Head Penetration Inspections, Boric Acid Corrosion Control


====a. Inspection Scope====
====a. Inspection Scope====
The inspectors:
The procedure requires review of two or three types of nondestructive examination (NDE) activities (volumetric, surface, and visual.) The inspector reviewed multiple examples of all three types.
: (1) reviewed plant procedures, calculations, the FSAR Update, Technical Specifications (TSs), and vendor manuals to determine the impact of ultra-low


sulfur diesel fuel on the capability of the diesel engine generators;
The procedure requires review of one or two ex aminations from the previous outage with recordable indications that were accepted for continued service. The inspector reviewed
: (2) reviewed


outstanding design issues, operator workarounds, and FSAR Update documents to
one such examination (Residual Heat Removal System Piping Weld RB-119-II).


determine if open issues affected the functionality of the diesel engine generators; and
If PG&E completed welding on the pressure boundary for Class 1 or 2 systems since the beginning of the previous outage, the procedure requires verification for one-to-three
: (3) verified that Pacific Gas and Electric Company (PG&E) was identifying and resolving


equipment alignment problems. Documents revi ewed by the inspectors are listed in the attachment.
welds that acceptance and preservice examinations were done in accordance with


The inspectors completed one sample.
American Society of Mechanical Engineers (ASME) Code. The inspector verified one


====b. Findings====
such weld (Safety Injection System Weld 2SI-119-8III).The procedure requires verification that one or two ASME Section XI Code repairs orreplacements meet Code requirements. The inspector verified two Section XI repairs (replacement of Component Cooling Water Valves 2-279 and 2-280 and replacement of
No findings of significance were identified.
{{a|1R05}}
==1R05 Fire Protection (71111.05)==


===.1 Quarterly Inspection===
Residual Heat Removal Valve 2-8742B).


====a. Inspection Scope====
The inspector verified, through direct observation or record review, that ultrasonic, eddy current, liquid penetrant, radiographic, or visual examinations of the components listed
The inspectors walked down the six below listed plant areas to assess the material condition of active and passive fire protection features and their operational lineup and


readiness. The inspectors:
below were performed in accordance with ASME Code requirements.
: (1) verified that transient combustibles and hot work


activities were controlled in accordance with plant procedures;
-11-System Component/Weld Identification Examination MethodFeedwaterSteam Generator 1 Feedwater Supply Hanger 2037-7V Visual (VT-3)
: (2) observed the
Auxiliary Feedwater (AFW)
AFW Pump 2-1 Discharge Header Hanger 414-505R Visual (VT-3)AFWAFW Pump 2-1 Discharge Header Hanger 414-386R Visual (VT-3)AFWAFW Supply Hanger 42-42RVisual (VT-3)
Chemical Volume Control SystemCVCS-2-8388C, FW-2RadiographicFeedwaterK16-555-16/Integral AttachmentsMagnetic Particle &
UltrasonicFeedwaterK16-557-16Magnetic Particle &
UltrasonicReactor CoolantS6-959-2 SPL WIB-503Liquid Penetrant Reactor CoolantS6-959-2 SPL WIB-1009Liquid Penetrant Reactor VesselCircumferential Weld 9-201Ultrasonic Reactor VesselLoop 2 Outlet Safe-endUltrasonic During the review of each examination, the inspector verified that the correct NDE procedures were used, that examinations and conditions were as specified in the


condition of fire detection devices to verify they remained functional;
procedure, and that test instrumentation or equipment was properly calibrated and within
: (3) observed fire


suppression systems to verify they re mained functional and that access to manual actuators was unobstructed;
the allowable calibration period. The inspector also reviewed documentation such as
: (4) verified that fire extinguishers and hose stations were


provided at their designated locations and that they were in a satisfactory condition;
ultrasonic and eddy current inspection records to determine if the indications revealed by
: (5) verified that passive fire protection features (electrical raceway barriers, fire doors, fire dampers, steel fire proofing, penetration seals, and oil collection systems) were in a


satisfactory material condition;
the examinations were compared against the ASME Code specified acceptance
: (6) verified that adequate compensatory measures were


established for degraded or inoperable fire protection features and that the
standards. This review also determined that indications were appropriately


compensatory measures were commensurate with the significance of the deficiency; and
dispositioned.
: (7) reviewed the FSAR Update to determine if PG&E identified and corrected fire


protection problems.*April 10, 2006:  Unit 2, 140 foot turbine building
The inspector verified the NDE certifications of those personnel observed performing examinations or identified during review of completed examination packages.
-9-*April 14, 2006:  Unit 2, 64 foot auxiliary building*May 1, 2006:  Units 1 and 2, intake structure
 
*May 2, 2006:  Unit 2, Containment Fire Zones 1A, 1B, and 1C
The inspector also reviewed the replacement of four valves performed in accordancewith ASME Section XI. During the replacement of two component cooling water valves
*May 2, 2006:  Unit 1, 85 foot auxiliary building
-12-that supply cooling to the reactor vessel support pads, the inspector found that PG&E did not verify the minimum preheat temperature prior to welding.
*May 8, 2006: Security diesel engine generator building Documents reviewed by the inspectors are listed in the attachment.


The inspectors completed six samples.
The minimum sample requirements of the inspection procedure were satisfied.


====b. Findings====
====b. Findings====
No findings of significance were identified.
Introduction
{{a|1R06}}
:  A Green, noncited violation (NCV) of TS 5.4.1.a was identified for failure to follow the procedure for ensuring that welding preheat temperatures were verified prior
==1R06 Flood Protection Measures (71111.06)==
 
to welding. Specifically, on April 26, 2006, during the replacement of Component


Annual External Flooding
Cooling Water Valves 279 and 280, which provide cooling to the reactor vessel support


====a. Inspection Scope====
pads, PG&E failed to verify that the minimum welding preheat temperature of 50°F was
The inspectors:
: (1) reviewed the FSAR Update, the flooding analysis, and plant procedures to assess seasonal susceptibilities involving external flooding;
: (2) reviewed


the FSAR Update and CAP to determine if PG&E identified and corrected flooding
met and PG&E could not demonstrate that the ambient temperature was greater than


problems;
50°F. Description
: (3) inspected underground bunkers/manholes to verify the adequacy of:
: The replacement of Valves 279 and 280 was performed in accordance with Work Order CO196956, which referenced Welding Procedure Specification 5, "Welding
: (a) sump pumps,
 
: (b) level alarm circuits,
of P1 Materials with GTAW and/or SMAW," Revision 8; Nuclear Welding Control Manual
: (c) cable splices subject to submergence, and
: (d) drainage for bunkers/manholes;
: (4) verified that operator actions for coping with


flooding can reasonably achieve the desired outcomes; and
Procedures GWS-ASME,"ASME General Welding Standard," Revision 8; and WI-1, "Visual Inspection of Welds," Revision 7. Welding Procedure Specification 5 lists a
: (5) walked down the one


below listed area to verify the adequacy of:
minimum preheat temperature of 50°F as an essential variable. Section 4.5 of
: (a) equipment seals located below the


floodline,
GWS-ASME states that preheat temperature shall be verified with thermocouples or
: (b) floor and wall penetration seals,
: (c) watertight door seals,
: (d) common drain


lines and sumps,
temperature indicating crayons or contact pyrometers outside the weld joint but near the
: (e) sump pumps, level alarms, and control circuits, and
: (f) temporary or


removable flood barriers.*April 2, 2006:  Units 1 and 2, 500 kV switchyard Pullboxes W-3 and W-4
weld area. Section 6.7 of Procedure WI-1 states that verification of preheat temperature


Documents reviewed by the inspectors are listed in the attachment.
is not mandatory for welds that require a minimum preheat of 50°F, if it can be


The inspectors completed one sample.
demonstrated that the ambient temperature is greater than 50°F. During the


====b. Findings====
replacement of Valves 279 and 280, PG&E did not verify the preheat temperature prior
No findings of significance were identified.
{{a|1R07}}
==1R07 Heat Sink Performance (71111.07)==


====a. Inspection Scope====
to welding. The containment building was open to the environment and no ambient
The inspectors reviewed PG&E's programs, verified performance against industry standards, and reviewed critical operating parameters and maintenance records for


Component Cooling Water Heat Exchangers 1-1 and 1-2. The inspectors verified that:
temperature measurement was performed to demonstrate that the ambient temperature was greater than 50°F.
-10-(1) performance tests were satisfactorily conducted for heat exchangers/heat sinks and reviewed for problems or errors;
: (2) PG&E utilized the periodic maintenance method


outlined in Electric Power Research Institute NP-7552, "Heat Exchanger Performance
=====Analysis:=====
The performance deficiency associated with this finding is a failure to follow procedures. This deficiency impacted the Barrier Integrity Cornerstone and, as


Monitoring Guidelines;"
described in Inspection Manual Chapter (IMC) 0612, Appendix B, the finding was
: (3) PG&E properly utilized biofouling controls;
: (4) PG&E's heat


exchanger inspections adequately assessed the state of cleanliness of their tubes, and
considered more than minor since it affected the cornerstone objective of providing
: (5) the heat exchanger was correctly categorized under the Maintenance Rule.


Documents reviewed by the inspectors included Procedure PEP -234, "CCW Heat Exchanger Performance Test," Revision 9.
reasonable assurance that physical design barriers, in this case the RCS, protect the


The inspectors completed one sample.
public from radionuclide releases caused by a ccidents or events. Specifically, the failure to ensure minimum preheat temperature prior to welding affected the cornerstone


====b. Findings====
attribute of human performance and its impact on maintaining functionality of the RCS
No findings of significance were identified.
{{a|1R08}}
==1R08 Inservice Inspection Activities (71111.08)==


===.1 Inspection Activities Other Than Steam Generator Tube Inspections, Pressurized Water===
because not adequately controlling the welding process can lead to weld failures.
 
Minimum preheat temperature is defined in Section IX of the ASME Code as an


Reactor Vessel Upper Head Penetration Inspections, Boric Acid Corrosion Control
essential variable which can affect the mechanical properties of a weldment. For carbon


====a. Inspection Scope====
steels or low alloy steels, the failure to observe the specified minimum preheat
The procedure requires review of two or three types of nondestructive examination (NDE) activities (volumetric, surface, and visual.)  The inspector reviewed multiple examples of all three types.


The procedure requires review of one or two ex aminations from the previous outage with recordable indications that were accepted for continued service. The inspector reviewed
temperature could result in too rapid cooling and the formation of martensite, a brittle


one such examination (Residual Heat Removal System Piping Weld RB-119-II).
structure. Rapid cooling could also impede the ability of the weldment to evolve gases


If PG&E completed welding on the pressure boundary for Class 1 or 2 systems since the beginning of the previous outage, the procedure requires verification for one-to-three
introduced or formed during the welding operation, leading to hydrogen embrittlement.


welds that acceptance and preservice examinations were done in accordance with
The finding was determined to be of very low safety significance based on management


American Society of Mechanical Engineers (ASME) Code. The inspector verified one
review of the plant conditions at the time the performance deficiency occurred (defueled)


such weld (Safety Injection System Weld 2SI-119-8III).The procedure requires verification that one or two ASME Section XI Code repairs orreplacements meet Code requirements. The inspector verified two Section XI repairs (replacement of Component Cooling Water Valves 2-279 and 2-280 and replacement of
and the condition was evaluated prior to the plant entering Mode 5.


Residual Heat Removal Valve 2-8742B).
-13-Enforcement
:  TS 5.4.1.a requires that written procedures shall be established, implemented, and maintained covering the applicable procedures recommended in


The inspector verified, through direct observation or record review, that ultrasonic, eddy current, liquid penetrant, radiographic, or visual examinations of the components listed
Appendix A of Regulatory Guide 1.33, Revision 2, Appendix A, February 1978.


below were performed in accordance with ASME Code requirements.
Appendix A, Section 9, lists procedures for performing maintenance activities, such as


-11-System Component/Weld Identification Examination MethodFeedwaterSteam Generator 1 Feedwater Supply Hanger 2037-7V Visual (VT-3)
welding. Welding Procedure Specification 5 and Nuclear Welding Control Manual
Auxiliary Feedwater (AFW)
AFW Pump 2-1 Discharge Header Hanger 414-505R Visual (VT-3)AFWAFW Pump 2-1 Discharge Header Hanger 414-386R Visual (VT-3)AFWAFW Supply Hanger 42-42RVisual (VT-3)
Chemical Volume Control SystemCVCS-2-8388C, FW-2RadiographicFeedwaterK16-555-16/Integral AttachmentsMagnetic Particle &
UltrasonicFeedwaterK16-557-16Magnetic Particle &
UltrasonicReactor CoolantS6-959-2 SPL WIB-503Liquid Penetrant Reactor CoolantS6-959-2 SPL WIB-1009Liquid Penetrant Reactor VesselCircumferential Weld 9-201Ultrasonic Reactor VesselLoop 2 Outlet Safe-endUltrasonic During the review of each examination, the inspector verified that the correct NDE procedures were used, that examinations and conditions were as specified in the


procedure, and that test instrumentation or equipment was properly calibrated and within
Procedures GWS-ASME and WI-1 require that minimum preheat temperature be verified


the allowable calibration period. The inspector also reviewed documentation such as
prior to welding. Contrary to the above, on April 24, 2006, PG&E failed to follow these


ultrasonic and eddy current inspection records to determine if the indications revealed by
procedures by not verifying the preheat tem perature nor that the ambient temperature was above 50°F before beginning welding on Component Cooling Water Valves 279


the examinations were compared against the ASME Code specified acceptance
and 280. Because the failure to follow procedures was of very low safety significance


standards. This review also determined that indications were appropriately
and has been entered into the CAP as Action Request (AR) A0665588, this violation is


dispositioned.
being treated as an noncited violation, consistent with Section VI.A of the NRC


The inspector verified the NDE certifications of those personnel observed performing examinations or identified during review of completed examination packages.
Enforcement Policy:  NCV 50-323/06-03-01, Failure to Follow Procedures for Welding.


The inspector also reviewed the replacement of four valves performed in accordancewith ASME Section XI. During the replacement of two component cooling water valves
===.2 Pressurized Water Reactor Vessel Upper Head Penetration Inspection Activities===
-12-that supply cooling to the reactor vessel support pads, the inspector found that PG&E did not verify the minimum preheat temperature prior to welding.


The minimum sample requirements of the inspection procedure were satisfied.
====a. Inspection Scope====
The inspector reviewed PG&E's reactor vessel upper head penetration (VUHP) nozzle inspection activities implemented in accordance with the requirements of NRC


====b. Findings====
Order EA-03-009, issued on February 20, 2004. PG&E's nonvisual NDE technique was
Introduction
:  A Green, noncited violation (NCV) of TS 5.4.1.a was identified for failure to follow the procedure for ensuring that welding preheat temperatures were verified prior


to welding. Specifically, on April 26, 2006, during the replacement of Component
a surface examination using ultrasonic and eddy current testing of the wetted surface of


Cooling Water Valves 279 and 280, which provide cooling to the reactor vessel support
the VUHP nozzle base material and the J-groove weld.


pads, PG&E failed to verify that the minimum welding preheat temperature of 50°F was
The inspector observed a sample of NDE performed on the vessel head from remote video feeds at the collection and analysis stations. The inspector examined ultrasonic


met and PG&E could not demonstrate that the ambient temperature was greater than
and eddy current data collected. A review of the NDE examination procedures used was


50°F. Description
also performed to confirm that they were consistent with the ASME Code and that the
:  The replacement of Valves 279 and 280 was performed in accordance with Work Order CO196956, which referenced Welding Procedure Specification 5, "Welding


of P1 Materials with GTAW and/or SMAW," Revision 8; Nuclear Welding Control Manual
equipment and calibration requirements were consistent with that used in mockup


Procedures GWS-ASME,"ASME General Welding Standard," Revision 8; and WI-1, "Visual Inspection of Welds," Revision 7. Welding Procedure Specification 5 lists a
demonstrations on simulated actual cracking. The inspector also reviewed records


minimum preheat temperature of 50°F as an essential variable. Section 4.5 of
indicating the extent of inspection for each penetration nozzle, including documents


GWS-ASME states that preheat temperature shall be verified with thermocouples or
which resolved interference or masking issues. Specifically, the inspector verified that


temperature indicating crayons or contact pyrometers outside the weld joint but near the
PG&E achieved ultrasonic testing coverage to the maximum extent possible. In all


weld area. Section 6.7 of Procedure WI-1 states that verification of preheat temperature
cases, the coverage was from 2 inches above the J-groove weld down to the lowest


is not mandatory for welds that require a minimum preheat of 50°F, if it can be
elevation that could be practically inspected on each nozzle with the ultrasonic testing


demonstrated that the ambient temperature is greater than 50°F. During the
probe being used with a minimum required inspection distance of 0.3 inches below the


replacement of Valves 279 and 280, PG&E did not verify the preheat temperature prior
J-groove weld. This criteria was specified in an NRC approved alternate examination


to welding. The containment building was open to the environment and no ambient
criteria for 78 VUHP nozzles.


temperature measurement was performed to demonstrate that the ambient temperature was greater than 50°F.
For all activities reviewed, the inspector determined that the activities were performed in accordance with the requirements of the NRC Order. No indications or defects were


=====Analysis:=====
detected. There had not been any indications previously identified which had been
The performance deficiency associated with this finding is a failure to follow procedures. This deficiency impacted the Barrier Integrity Cornerstone and, as


described in Inspection Manual Chapter (IMC) 0612, Appendix B, the finding was
accepted for continued service.


considered more than minor since it affected the cornerstone objective of providing
The minimum sample requirements of the inspection procedure were satisfied.


reasonable assurance that physical design barriers, in this case the RCS, protect the
====b. Findings====
No findings of significance were identified.


public from radionuclide releases caused by a ccidents or events. Specifically, the failure to ensure minimum preheat temperature prior to welding affected the cornerstone
-14-


attribute of human performance and its impact on maintaining functionality of the RCS
===.3 Boric Acid Corrosion Control Inspection Activities (Pressurized Water Reactors)===


because not adequately controlling the welding process can lead to weld failures.
====a. Inspection Scope====
The inspector reviewed a sample of boric acid corrosion control walkdown visual examination activities. The inspector determined that PG&E's visual inspections


Minimum preheat temperature is defined in Section IX of the ASME Code as an
emphasized locations where boric acid leaks could cause degradation of safety


essential variable which can affect the mechanical properties of a weldment. For carbon
significant components.


steels or low alloy steels, the failure to observe the specified minimum preheat
The inspector reviewed three engineering evaluations performed for boric acid found on RCS piping and components. The review verified that ASME Code wall thickness


temperature could result in too rapid cooling and the formation of martensite, a brittle
requirements were maintained and that the degraded conditions were properly entered


structure. Rapid cooling could also impede the ability of the weldment to evolve gases
and dispositioned in PG&E's CAP.


introduced or formed during the welding operation, leading to hydrogen embrittlement.
The minimum sample requirements of the inspection procedure were satisfied.


The finding was determined to be of very low safety significance based on management
====b. Findings====
No findings of significance were identified.


review of the plant conditions at the time the performance deficiency occurred (defueled)
===.4 Steam Generator Tube Inspection Activities===


and the condition was evaluated prior to the plant entering Mode 5.
====a. Inspection Scope====
The inspector verified that the steam generator tube eddy current examination scope and expansion criteria met the TS requirements, industry guidelines, and commitments


-13-Enforcement
made to the NRC. The inspector confirmed that known areas of potential degradation
:  TS 5.4.1.a requires that written procedures shall be established, implemented, and maintained covering the applicable procedures recommended in


Appendix A of Regulatory Guide 1.33, Revision 2, Appendix A, February 1978.
based on site-specific and industry experience were included in the scope of the


Appendix A, Section 9, lists procedures for performing maintenance activities, such as
inspection. The inspector observed the collection and analysis of eddy current data by


welding. Welding Procedure Specification 5 and Nuclear Welding Control Manual
contractor personnel and verified that:
: (1) the eddy current probes being utilized were


Procedures GWS-ASME and WI-1 require that minimum preheat temperature be verified
appropriate for identifying the expected types of indications,
: (2) probe position location


prior to welding. Contrary to the above, on April 24, 2006, PG&E failed to follow these
verification was being performed,
: (3) calibration requirements were being adhered to, and
: (4) probe travel speed was in accordance with procedural requirements.


procedures by not verifying the preheat tem perature nor that the ambient temperature was above 50°F before beginning welding on Component Cooling Water Valves 279
The inspector verified that PG&E compared flaws detected during the current outage against the previous outage data and that appropriate repair criteria was specified. One


and 280. Because the failure to follow procedures was of very low safety significance
hundred percent of all steam generator tubes were inspected during this outage. The


and has been entered into the CAP as Action Request (AR) A0665588, this violation is
inspector noted that the number of tubes required to be plugged was consistent with


being treated as an noncited violation, consistent with Section VI.A of the NRC
predictions made prior to the start of the outage. Tube plugging activities during the


Enforcement Policy:  NCV 50-323/06-03-01, Failure to Follow Procedures for Welding.
inspection were in accordance with procedural requirements and were within the


===.2 Pressurized Water Reactor Vessel Upper Head Penetration Inspection Activities===
allowable limits for tube plugging.


====a. Inspection Scope====
The minimum sample requirements of the inspection procedure were satisfied.
The inspector reviewed PG&E's reactor vessel upper head penetration (VUHP) nozzle inspection activities implemented in accordance with the requirements of NRC


Order EA-03-009, issued on February 20, 2004. PG&E's nonvisual NDE technique was
====b. Findings====
No findings of significance were identified.
{{a|1R11}}
==1R11 Licensed Operator Requalification (71111.11)==


a surface examination using ultrasonic and eddy current testing of the wetted surface of
-15-


the VUHP nozzle base material and the J-groove weld.
===.1 Quarterly Inspection===


The inspector observed a sample of NDE performed on the vessel head from remote video feeds at the collection and analysis stations. The inspector examined ultrasonic
====a. Inspection Scope====
The inspectors observed testing and training of senior reactor operators and reactor operators to identify deficiencies and discrepancies in the training, to assess operator


and eddy current data collected. A review of the NDE examination procedures used was
performance, and to assess the evaluator's critique. The training scenario involved a


also performed to confirm that they were consistent with the ASME Code and that the
positive displacement pump overcurrent trip , loss of a vital 4 kV bus, an earthquake, and an anticipated transient without scram.


equipment and calibration requirements were consistent with that used in mockup
Documents reviewed by the inspectors included Lesson FRS1-A, Attachment 2,"Simulator Event Sequence," Revision 14.


demonstrations on simulated actual cracking. The inspector also reviewed records
The inspectors completed one sample.


indicating the extent of inspection for each penetration nozzle, including documents
====b. Findings====
No findings of significance were identified.


which resolved interference or masking issues. Specifically, the inspector verified that
===.2 Biennial Inspection===


PG&E achieved ultrasonic testing coverage to the maximum extent possible. In all
====a. Inspection Scope====
Following the completion of the annual operating examination testing cycle, which ended the week of April 4, 2006, the inspectors reviewed the overall pass/fail results of the


cases, the coverage was from 2 inches above the J-groove weld down to the lowest
annual individual job performance measure operating tests and simulator operating tests


elevation that could be practically inspected on each nozzle with the ultrasonic testing
administered by PG&E staff during the operator licensing requalification cycle. Sixteen


probe being used with a minimum required inspection distance of 0.3 inches below the
separate crews participated in simulator operating tests, and 79 licensed operators took


J-groove weld. This criteria was specified in an NRC approved alternate examination
the job performance measure operating tests. All of the crews tested passed the


criteria for 78 VUHP nozzles.
simulator portion of the annual operating test. All of the licensed operators, except one, passed the job performance measure portion of the examination. The licensed operator


For all activities reviewed, the inspector determined that the activities were performed in accordance with the requirements of the NRC Order. No indications or defects were  
was successfully remediated prior to returning to shift. These results were compared to


detected. There had not been any indications previously identified which had been
the thresholds established in IMC 609, Appendix I, "Operator Requalification Human


accepted for continued service.
Performance Significance Determination Process." The inspectors completed one sample.
 
The minimum sample requirements of the inspection procedure were satisfied.


====b. Findings====
====b. Findings====
No findings of significance were identified.
No findings of significance were identified.
{{a|1R12}}
==1R12 Maintenance Effectiveness (71111.12)==


-14-
====a. Inspection Scope====
The inspectors reviewed the one below listed maintenance activity to:
: (1) verify the appropriate handling of structure, system, and component (SSC) performance or


===.3 Boric Acid Corrosion Control Inspection Activities (Pressurized Water Reactors)===
condition problems;
: (2) verify the appropriate handling of degraded SSC functional


====a. Inspection Scope====
performance;
The inspector reviewed a sample of boric acid corrosion control walkdown visual examination activities. The inspector determined that PG&E's visual inspections
: (3) evaluate the role of work practices and common cause problems; and
-16-(4) evaluate the handling of SSC issues reviewed under the requirements of the Maintenance Rule, 10 CFR Part 50, Appendix B, and the TSs.*May 1, 2006:  Units 1 and 2, Containment isolation valves


emphasized locations where boric acid leaks could cause degradation of safety
Documents reviewed by the inspectors are listed in the attachment.


significant components.
The inspectors completed one sample.
 
The inspector reviewed three engineering evaluations performed for boric acid found on RCS piping and components. The review verified that ASME Code wall thickness
 
requirements were maintained and that the degraded conditions were properly entered
 
and dispositioned in PG&E's CAP.
 
The minimum sample requirements of the inspection procedure were satisfied.


====b. Findings====
====b. Findings====
No findings of significance were identified.
No findings of significance were identified.
{{a|1R13}}
==1R13 Maintenance Risk Assessments and Emergent Work Control (71111.13)==


===.4 Steam Generator Tube Inspection Activities===
===.1 Risk Assessments and Management of Risk===


====a. Inspection Scope====
====a. Inspection Scope====
The inspector verified that the steam generator tube eddy current examination scope and expansion criteria met the TS requirements, industry guidelines, and commitments
The inspectors reviewed the one below listed assessment activities to verify:
: (1) performance of risk assessments when required by 10 CFR 50.65(a)(4) and PG&E


made to the NRC. The inspector confirmed that known areas of potential degradation
procedures prior to changes in plant configuration for maintenance activities and plant


based on site-specific and industry experience were included in the scope of the
operations;
: (2) the accuracy, adequacy, and completeness of the information considered


inspection. The inspector observed the collection and analysis of eddy current data by
in the risk assessment;
: (3) that PG&E recognizes, and/or enters as applicable, the


contractor personnel and verified that:
appropriate risk category according to the risk assessment results and PG&E
: (1) the eddy current probes being utilized were


appropriate for identifying the expected types of indications,
procedures; and
: (2) probe position location
: (4) that PG&E identified and corrected problems related to maintenance risk assessments.*April 5, 2006:  Unit 2; Diesel Fuel Oil Transfer Pump 0-1 and Electrohydraulic Pump 2-2 preventive maintenance, 500 kV Circuit Breaker 542 replacement, and


verification was being performed,
Morro Bay to Diablo Canyon 230 kV line outage due to fiber optic cable
: (3) calibration requirements were being adhered to, and
: (4) probe travel speed was in accordance with procedural requirements.


The inspector verified that PG&E compared flaws detected during the current outage against the previous outage data and that appropriate repair criteria was specified. One
installation.


hundred percent of all steam generator tubes were inspected during this outage. The
Documents reviewed by the inspectors included Procedure AD7.DC6, "On-line Maintenance Risk Management," Revision 9.


inspector noted that the number of tubes required to be plugged was consistent with
The inspectors completed one sample.


predictions made prior to the start of the outage. Tube plugging activities during the
====b. Findings====
No findings of significance were identified.


inspection were in accordance with procedural requirements and were within the
===.2 Emergent Work===


allowable limits for tube plugging.
====a. Inspection Scope====
The inspectors:
: (1) verified that PG&E performed actions to minimize the probability of initiating events and maintained the functional capability of mitigating systems and


The minimum sample requirements of the inspection procedure were satisfied.
barrier integrity systems;
: (2) verified that emergent work-related activities such as
-17-troubleshooting, work planning/scheduling, establishing plant conditions, aligning equipment, tagging, temporary modifications, and equipment restoration did not place


====b. Findings====
the plant in an unacceptable configuration; and
No findings of significance were identified.
: (3) reviewed the FSAR Update to
{{a|1R11}}
==1R11 Licensed Operator Requalification (71111.11)==


-15-
determine if PG&E identified and corrected risk assessment and emergent work control


===.1 Quarterly Inspection===
problems.*April 2, 2006:  Unit 1, Diesel Engine Generator 1-3 voltage regulator failure
*June 3, 2006:  Unit 1, Failure of rod control system to manually withdraw Bank D control rods from core Documents reviewed by the inspectors are listed in the attachment.


====a. Inspection Scope====
The inspectors completed two samples.
The inspectors observed testing and training of senior reactor operators and reactor operators to identify deficiencies and discrepancies in the training, to assess operator
 
performance, and to assess the evaluator's critique. The training scenario involved a
 
positive displacement pump overcurrent trip , loss of a vital 4 kV bus, an earthquake, and an anticipated transient without scram.
 
Documents reviewed by the inspectors included Lesson FRS1-A, Attachment 2,"Simulator Event Sequence," Revision 14.
 
The inspectors completed one sample.


====b. Findings====
====b. Findings====
No findings of significance were identified.
No findings of significance were identified.
 
{{a|1R14}}
===.2 Biennial Inspection===
==1R14 Personnel Performance Related to Nonroutine Plant Evolutions and Events (71111.14)==


====a. Inspection Scope====
====a. Inspection Scope====
Following the completion of the annual operating examination testing cycle, which ended the week of April 4, 2006, the inspectors reviewed the overall pass/fail results of the
The inspectors:
: (1) reviewed operator logs, plant computer data, and/or strip charts for the below listed evolutions to evaluate operator performance in coping with nonroutine


annual individual job performance measure operating tests and simulator operating tests
events and transients;
: (2) verified that operator actions were in accordance with the


administered by PG&E staff during the operator licensing requalification cycle. Sixteen
response required by plant procedures and training; and
: (3) verified that PG&E has


separate crews participated in simulator operating tests, and 79 licensed operators took
identified and implemented appropriate corrective actions associated with personnel


the job performance measure operating tests. All of the crews tested passed the
performance problems that occurred during the nonroutine evolutions sampled.*April 23, 2006:  Unit 2, Fuel handling cart position resolver failed while a fuelassembly was in motion*May 4, 2006:  Units 1 and 2, Magnitude 2.8 earthquake approximately 6 km west northwest of Diablo Canyon Power Plant*May 25, 2006:  Unit 2, Auxiliary Transformer 2-1 sudden pressure trip


simulator portion of the annual operating test. All of the licensed operators, except one, passed the job performance measure portion of the examination. The licensed operator
Documents reviewed by the inspectors are listed in the attachment.


was successfully remediated prior to returning to shift. These results were compared to
The inspectors completed three samples.
 
the thresholds established in IMC 609, Appendix I, "Operator Requalification Human
 
Performance Significance Determination Process." The inspectors completed one sample.


====b. Findings====
====b. Findings====
No findings of significance were identified.
No findings of significance were identified.
{{a|1R12}}
{{a|1R15}}
==1R12 Maintenance Effectiveness (71111.12)==
==1R15 Operability Evaluations (71111.15)==


====a. Inspection Scope====
====a. Inspection Scope====
The inspectors reviewed the one below listed maintenance activity to:
-18-The inspectors:
: (1) verify the appropriate handling of structure, system, and component (SSC) performance or
: (1) reviewed plant status documents, such as operator shift logs, emergent work documentation, deferred modifications, and standing orders, to


condition problems;
determine if an operability evaluation was warranted for degraded components;
: (2) verify the appropriate handling of degraded SSC functional
: (2) referred to the FSAR Update and design bases documents to review the technical


performance;
adequacy of the operability evaluations;
: (3) evaluate the role of work practices and common cause problems; and
: (3) evaluated compensatory measures
-16-(4) evaluate the handling of SSC issues reviewed under the requirements of the Maintenance Rule, 10 CFR Part 50, Appendix B, and the TSs.*May 1, 2006:  Units 1 and 2, Containment isolation valves


Documents reviewed by the inspectors are listed in the attachment.
associated with operability evaluations;
: (4) determined degraded component impact on


The inspectors completed one sample.
any TS;
: (5) used the significance determination process to evaluate the risk significance


====b. Findings====
of degraded or inoperable equipment; and
No findings of significance were identified.
: (5) verified that PG&E has identified and
{{a|1R13}}
==1R13 Maintenance Risk Assessments and Emergent Work Control (71111.13)==


===.1 Risk Assessments and Management of Risk===
implemented appropriate corrective actions associated with degraded components.*April 14, 2006:  Unit 1, Condensate storage tank epoxy delamination*April 14, 2006:  Unit 2, Residual heat removal system weld flaw
*May 8, 2006:  Unit 2, Station vital inverters
*May 9, 2006:  Units 1 and 2, Feedwater ultrasonic flow meter data scatter
*May 21, 2006: Unit 2, Accumulator 2-3 discharge line water hammer Documents reviewed by the inspectors are listed in the attachment.


====a. Inspection Scope====
The inspectors completed five samples.
The inspectors reviewed the one below listed assessment activities to verify:
: (1) performance of risk assessments when required by 10 CFR 50.65(a)(4) and PG&E


procedures prior to changes in plant configuration for maintenance activities and plant
====b. Findings====


operations;
=====Introduction:=====
: (2) the accuracy, adequacy, and completeness of the information considered
A self-revealing, NCV of 10 CFR Part 50, Appendix B, Criterion XVI, was determined for the failure of operators to promptly identify a condition adverse to quality.


in the risk assessment;
Specifically, operators failed to document in the CAP an unexpected level drop in
: (3) that PG&E recognizes, and/or enters as applicable, the


appropriate risk category according to the risk assessment results and PG&E
Accumulator 1-3 during Refueling Outage 1R13. Failure to enter the occurrence into the


procedures; and
CAP precluded corrective actions that would have prevented the unexpected level drop
: (4) that PG&E identified and corrected problems related to maintenance risk assessments.*April 5, 2006:  Unit 2; Diesel Fuel Oil Transfer Pump 0-1 and Electrohydraulic Pump 2-2 preventive maintenance, 500 kV Circuit Breaker 542 replacement, and


Morro Bay to Diablo Canyon 230 kV line outage due to fiber optic cable
in Accumulator 2-3 and the water hammer of its discharge piping.


installation.
Description
:  On May 21, 2006, with Unit 2 in Mode 4 and reactor coolant system pressure at 935 psig, operators opened Accumulator 2-3 Discharge Valve SI-2-8808C


Documents reviewed by the inspectors included Procedure AD7.DC6, "On-line Maintenance Risk Management," Revision 9.
and subsequently Accumulator 2-3 level unexpectedly dropped from 67 to 57 percent.


The inspectors completed one sample.
At the same time, operators received a Reactor Coolant Pump 2-3 vibration alarm and


====b. Findings====
audible indications of a water hammer from inside containment. PG&E staff concluded
No findings of significance were identified.


===.2 Emergent Work===
that a water hammer had occurred inside the discharge piping of Accumulator 2-3. As


====a. Inspection Scope====
immediate corrective actions, PG&E staff visually walked down Accumulator 2-3
The inspectors:
: (1) verified that PG&E performed actions to minimize the probability of initiating events and maintained the functional capability of mitigating systems and


barrier integrity systems;
discharge piping and supports, verified operability of the discharge piping seismic
: (2) verified that emergent work-related activities such as
-17-troubleshooting, work planning/scheduling, establishing plant conditions, aligning equipment, tagging, temporary modifications, and equipment restoration did not place


the plant in an unacceptable configuration; and
snubbers, and verified the absence of voids in other portions of Units 1 and 2 emergency
: (3) reviewed the FSAR Update to


determine if PG&E identified and corrected risk assessment and emergent work control
core cooling system piping. Upon review of Accumulator 2-3 piping layout, PG&E staff


problems.*April 2, 2006:  Unit 1, Diesel Engine Generator 1-3 voltage regulator failure
found that there were no vent points in the accumulator discharge piping between motor-
*June 3, 2006:  Unit 1, Failure of rod control system to manually withdraw Bank D control rods from core Documents reviewed by the inspectors are listed in the attachment.


The inspectors completed two samples.
operated discharge Valve SI-2-8808C and discharge check Valve SI-2-8956C.


====b. Findings====
Additionally, there were no procedures that specifically addressed the venting of the
No findings of significance were identified.
{{a|1R14}}
==1R14 Personnel Performance Related to Nonroutine Plant Evolutions and Events (71111.14)==


====a. Inspection Scope====
discharge line. The inspectors calculated approximately 83 feet of 10-inch pipe between
The inspectors:
: (1) reviewed operator logs, plant computer data, and/or strip charts for the below listed evolutions to evaluate operator performance in coping with nonroutine


events and transients;
the two valves, which equated to an approximate volume of 34.7 ft
: (2) verified that operator actions were in accordance with the


response required by plant procedures and training; and
===3. PG&E initiated a===
: (3) verified that PG&E has


identified and implemented appropriate corrective actions associated with personnel
root cause investigation under Nonconformance Report N0002207 to determine the


performance problems that occurred during the nonroutine evolutions sampled.*April 23, 2006:  Unit 2, Fuel handling cart position resolver failed while a fuelassembly was in motion*May 4, 2006:  Units 1 and 2, Magnitude 2.8 earthquake approximately 6 km west northwest of Diablo Canyon Power Plant*May 25, 2006:  Unit 2, Auxiliary Transformer 2-1 sudden pressure trip
cause(s) and appropriate corrective actions for the water hammer event.


Documents reviewed by the inspectors are listed in the attachment.
-19-While investigating the cause of the water hammer event, PG&E staff learned that a similar event had occurred with Accumulator 1-3 during Refueling Outage 1R13. On


The inspectors completed three samples.
November 27, 2005, operators opened Accumulator 1-3 Discharge Valve SI-1-8808C


====b. Findings====
and observed an approximate 7 percent level drop in the accumulator. However, there
No findings of significance were identified.
{{a|1R15}}
==1R15 Operability Evaluations (71111.15)==


====a. Inspection Scope====
were no corresponding indications of a water hammer, such as an audible noise or
-18-The inspectors:
: (1) reviewed plant status documents, such as operator shift logs, emergent work documentation, deferred modifications, and standing orders, to


determine if an operability evaluation was warranted for degraded components;
reactor coolant pump vibration alarms. Although the level drop was recorded in the
: (2) referred to the FSAR Update and design bases documents to review the technical


adequacy of the operability evaluations;
operator logs, operators failed to enter the unexpected occurrence into the CAP. PG&E
: (3) evaluated compensatory measures


associated with operability evaluations;
staff has since entered the occurrence as AR A0669453.
: (4) determined degraded component impact on


any TS;
The inspectors determined that the failure to address the Unit 1 accumulator level drop precluded corrective actions from being taken to prevent a recurrence of the event on
: (5) used the significance determination process to evaluate the risk significance


of degraded or inoperable equipment; and
Unit 2. Specifically, PG&E staff should have identified the voided condition after the
: (5) verified that PG&E has identified and


implemented appropriate corrective actions associated with degraded components.*April 14, 2006:  Unit 1, Condensate storage tank epoxy delamination*April 14, 2006:  Unit 2, Residual heat removal system weld flaw
Unit 1 accumulator level drop and that there was potential for voiding of the accumulator
*May 8, 2006:  Unit 2, Station vital inverters
*May 9, 2006:  Units 1 and 2, Feedwater ultrasonic flow meter data scatter
*May 21, 2006: Unit 2, Accumulator 2-3 discharge line water hammer Documents reviewed by the inspectors are listed in the attachment.


The inspectors completed five samples.
discharge piping due to the absence of vent points and procedures for venting.


====b. Findings====
=====Analysis:=====
The performance deficiency associated with this finding involved a failure of operations personnel to promptly identify a condition adverse to quality and enter it into


=====Introduction:=====
the CAP. The performance deficiency was self-revealing based on the second event
A self-revealing, NCV of 10 CFR Part 50, Appendix B, Criterion XVI, was determined for the failure of operators to promptly identify a condition adverse to quality.


Specifically, operators failed to document in the CAP an unexpected level drop in
initiating the licensee's review of the cause and subsequent identification that the event


Accumulator 1-3 during Refueling Outage 1R13. Failure to enter the occurrence into the
had occurred on Unit 1 also. The finding is greater than minor because it is associated


CAP precluded corrective actions that would have prevented the unexpected level drop
with the Mitigating Systems Cornerstone attribute of configuration control and affects the


in Accumulator 2-3 and the water hammer of its discharge piping.
associated cornerstone objective to ensure the availability, reliability, and capability of


Description
systems that respond to initiating events to prevent undesirable consequences. Using
:  On May 21, 2006, with Unit 2 in Mode 4 and reactor coolant system pressure at 935 psig, operators opened Accumulator 2-3 Discharge Valve SI-2-8808C


and subsequently Accumulator 2-3 level unexpectedly dropped from 67 to 57 percent.
the IMC 0609, "Significance Determination Process," Appendix A, Phase 1 Screening


At the same time, operators received a Reactor Coolant Pump 2-3 vibration alarm and
Worksheet, the finding is determined to be of very low safety significance because the


audible indications of a water hammer from inside containment. PG&E staff concluded
finding did not represent a loss of safety function, an actual loss of a safety-related train


that a water hammer had occurred inside the discharge piping of Accumulator 2-3. As
for greater than its TS allowed outage time, or screen as potentially risk-significant due


immediate corrective actions, PG&E staff visually walked down Accumulator 2-3
to seismic, fire, flooding, or severe weather initiating events. The finding had a


discharge piping and supports, verified operability of the discharge piping seismic
crosscutting aspect in the area of problem identification and resolution because


snubbers, and verified the absence of voids in other portions of Units 1 and 2 emergency
operations personnel failed to promptly identify, in the CAP, the unexpected level drop in


core cooling system piping. Upon review of Accumulator 2-3 piping layout, PG&E staff
Accumulator 1-3.


found that there were no vent points in the accumulator discharge piping between motor-
=====Enforcement:=====
10 CFR Part 50, Appendix B, Criterion XVI, "Corrective Action," requires, in part, that measures be established to assure that conditions adverse to quality are


operated discharge Valve SI-2-8808C and discharge check Valve SI-2-8956C.
promptly identified and corrected. Contrary to this, between November 27, 2005, and


Additionally, there were no procedures that specifically addressed the venting of the
May 24, 2006, operations personnel failed to assure that a condition adverse to quality


discharge line. The inspectors calculated approximately 83 feet of 10-inch pipe between
was promptly identified. Specifically, on November 27, 2005, the level in


the two valves, which equated to an approximate volume of 34.7 ft
Accumulator 1-3 unexpectedly dropped 7 percent when operators opened its discharge


===3. PG&E initiated a===
valve. Although operators documented the event in their logs, they failed to enter the


root cause investigation under Nonconformance Report N0002207 to determine the
occurrence into the CAP. Subsequently, no corrective actions were taken. On


cause(s) and appropriate corrective actions for the water hammer event.
May 21, 2006, when the discharge valve on Accumulator 2-3 was opened, its level


-19-While investigating the cause of the water hammer event, PG&E staff learned that a similar event had occurred with Accumulator 1-3 during Refueling Outage 1R13. On
unexpectedly dropped by 10 percent and a water hammer occurred in its discharge


November 27, 2005, operators opened Accumulator 1-3 Discharge Valve SI-1-8808C
piping. The apparent cause of the failure to promptly identify a condition adverse to


and observed an approximate 7 percent level drop in the accumulator. However, there
quality was that operators did not recognize the significance of the Accumulator 1-3 level


were no corresponding indications of a water hammer, such as an audible noise or
drop. Corrective actions include additional training of operations personnel regarding


reactor coolant pump vibration alarms. Although the level drop was recorded in the
the importance of promptly identifying conditions adverse to quality. Because the finding


operator logs, operators failed to enter the unexpected occurrence into the CAP. PG&E
is of very low safety significance and has been entered into PG&E's CAP as


staff has since entered the occurrence as AR A0669453.
AR A0669468, this violation is being treated as an NCV consistent with Section VI.A of
-20-the Enforcement Policy:  NCV 50-275/06-03-02, Failure to Promptly Identify Voiding in Accumulator Discharge Line.
{{a|1R17}}
==1R17 Permanent Plant Modifications (71111.17)==


The inspectors determined that the failure to address the Unit 1 accumulator level drop precluded corrective actions from being taken to prevent a recurrence of the event on
====a. Inspection Scope====
The inspectors reviewed key affected parameters associated with energy needs, materials/replacement components, timing, heat removal, control signals, equipment


Unit 2. Specifically, PG&E staff should have identified the voided condition after the
protection from hazards, operations, flowpaths, pressure boundary, ventilation boundary, structural, process medium properties, licensing basis, and failure modes for the one


Unit 1 accumulator level drop and that there was potential for voiding of the accumulator
modification listed below. The inspectors verified that:
: (1) modification preparation, staging, and implementation did not impair emergency/abnormal operating procedure


discharge piping due to the absence of vent points and procedures for venting.
actions, key safety functions, or operator response to loss of key safety functions;
: (2) postmodification testing maintained the plant in a safe configuration during testing by


=====Analysis:=====
verifying that unintended system interactions will not occur, SSC performance
The performance deficiency associated with this finding involved a failure of operations personnel to promptly identify a condition adverse to quality and enter it into


the CAP. The performance deficiency was self-revealing based on the second event
characteristics still met the design basis, the appropriateness of modification design


initiating the licensee's review of the cause and subsequent identification that the event
assumptions, and the modification test acceptance criteria has been met; and
: (3) PG&E


had occurred on Unit 1 also. The finding is greater than minor because it is associated
has identified and implemented appropriate corrective actions associated with


with the Mitigating Systems Cornerstone attribute of configuration control and affects the
permanent plant modifications. *May 19, 2006:  Removal of mesh over the residual heat removal suction point in the containment recirculation sump and modifications to the reactor cavity door to


associated cornerstone objective to ensure the availability, reliability, and capability of
address recirculation sump debris loading concerns Documents reviewed by the inspectors are listed in the attachment.


systems that respond to initiating events to prevent undesirable consequences. Using
The inspectors completed one sample.


the IMC 0609, "Significance Determination Process," Appendix A, Phase 1 Screening
====b. Findings====
No findings of significance were identified.
{{a|1R19}}
==1R19 Postmaintenance Testing (71111.19)==


Worksheet, the finding is determined to be of very low safety significance because the
====a. Inspection Scope====
The inspectors selected the nine below listed postmaintenance test activities of risk-significant systems or components. For each item, the inspectors:
: (1) reviewed the


finding did not represent a loss of safety function, an actual loss of a safety-related train
applicable licensing basis and/or design basis documents to determine the safety


for greater than its TS allowed outage time, or screen as potentially risk-significant due
functions;
: (2) evaluated the safety functions that may have been affected by the


to seismic, fire, flooding, or severe weather initiating events. The finding had a
maintenance activity; and
: (3) reviewed the test procedure to ensure it adequately tested


crosscutting aspect in the area of problem identification and resolution because
the safety function that may have been affected. The inspectors either witnessed or


operations personnel failed to promptly identify, in the CAP, the unexpected level drop in
reviewed test data to verify that acceptance criteria were met, plant impacts were


Accumulator 1-3.
evaluated, test equipment was calibrated, procedures were followed, jumpers were


=====Enforcement:=====
properly controlled, the test data results were complete and accurate, the test equipment
10 CFR Part 50, Appendix B, Criterion XVI, "Corrective Action," requires, in part, that measures be established to assure that conditions adverse to quality are


promptly identified and corrected. Contrary to this, between November 27, 2005, and
was removed, the system was properly realigned, and deficiencies during testing were


May 24, 2006, operations personnel failed to assure that a condition adverse to quality
documented. The inspectors also reviewed the FSAR Update to determine if PG&E


was promptly identified. Specifically, on November 27, 2005, the level in
identified and corrected problems related to postmaintenance testing.


Accumulator 1-3 unexpectedly dropped 7 percent when operators opened its discharge
-21-*April 18, 2006:  Unit 2, Containment Spray Pump 2-1 and 2-2*April 20, 2006:  Unit 2, Source Range Nuclear Instrument 31
*May 2, 2006:  Unit 2, Component Cooling Water Pump 2-3
*May 2, 2006:  Unit 2, Vital Inverter IY-21
*May 2, 2006:  Unit 2, 4kV Vital Bus "H" Switchgear
*May 5, 2006:  Unit 2, Auxiliary Saltwater Pump 2-2
*May 11, 2006:  Unit 2, Centrifugal Charging Pump 2-1
*May 12, 2006:  Unit 2, Fuel transfer cart position resolver
*May 18, 2006:  Unit 2, Auxiliary Transformer 2-1 Documents reviewed by the inspectors are listed in the attachment.


valve. Although operators documented the event in their logs, they failed to enter the
The inspectors completed nine samples.


occurrence into the CAP. Subsequently, no corrective actions were taken. On
====b. Findings====
No findings of significance were identified.
{{a|1R20}}
==1R20 Refueling and Outage Activities (71111.20)==


May 21, 2006, when the discharge valve on Accumulator 2-3 was opened, its level
====a. Inspection Scope====
The inspectors reviewed the following risk-significant refueling items or outage activities to verify defense-in-depth commensurate with the outage risk control plan, compliance


unexpectedly dropped by 10 percent and a water hammer occurred in its discharge
with the TS, and adherence to commitments in response to Generic Letter 88-17, "Loss


piping. The apparent cause of the failure to promptly identify a condition adverse to
of Decay Heat Removal":
: (1) the risk control plan;
: (2) tagging/clearance activities;
: (3) RCS instrumentation;
: (4) electrical power;
: (5) decay heat removal;
: (6) spent fuel pool


quality was that operators did not recognize the significance of the Accumulator 1-3 level
cooling;
: (7) inventory control;
: (8) reactivity control;
: (9) containment closure;
: (10) reduced


drop. Corrective actions include additional training of operations personnel regarding
inventory or midloop conditions;
: (11) refueling activities;
: (12) heatup and cooldown


the importance of promptly identifying conditions adverse to quality. Because the finding
activities;
: (13) restart activities; and
: (14) identification and implementation of appropriate


is of very low safety significance and has been entered into PG&E's CAP as
corrective actions associated with refueling and outage activities. The inspectors'


AR A0669468, this violation is being treated as an NCV consistent with Section VI.A of  
containment inspections included observations of the containment sump for damage and
-20-the Enforcement Policy:  NCV 50-275/06-03-02, Failure to Promptly Identify Voiding in Accumulator Discharge Line.
{{a|1R17}}
==1R17 Permanent Plant Modifications (71111.17)==


====a. Inspection Scope====
debris and supports, braces, and snubbers for evidence of excessive stress, water
The inspectors reviewed key affected parameters associated with energy needs, materials/replacement components, timing, heat removal, control signals, equipment


protection from hazards, operations, flowpaths, pressure boundary, ventilation boundary, structural, process medium properties, licensing basis, and failure modes for the one
hammer, or aging. Documents reviewed by the inspectors included the Unit 2 Refueling


modification listed below. The inspectors verified that:
Outage 2R13 Outage Safety Plan.
: (1) modification preparation, staging, and implementation did not impair emergency/abnormal operating procedure


actions, key safety functions, or operator response to loss of key safety functions;
The inspectors completed one sample.
: (2) postmodification testing maintained the plant in a safe configuration during testing by


verifying that unintended system interactions will not occur, SSC performance
====b. Findings====
Introduction
:  An NRC-identified NCV of TS 5.4.1.a was determined for an inadequate procedure, Procedure OP A-2:II, "Reactor Vessel - Draining the RCS to the Vessel


characteristics still met the design basis, the appropriateness of modification design
Flange - With Fuel in Vessel," Revision 33A. Specifically, the procedure did not address


assumptions, and the modification test acceptance criteria has been met; and
the reactor vessel level instrumentation required by the procedure deviated from actual
: (3) PG&E


has identified and implemented appropriate corrective actions associated with
level by approximately 15 inches when the time to boiling in the reactor vessel was


permanent plant modifications. *May 19, 2006:  Removal of mesh over the residual heat removal suction point in the containment recirculation sump and modifications to the reactor cavity door to
approximately 20 minutes, if shutdown cooling were lost.


address recirculation sump debris loading concerns Documents reviewed by the inspectors are listed in the attachment.
-22-Description
:  One action to ensure the integrity of shutdown cooling by operators was to prevent reactor vessel water level from dropping below the 107.5 foot elevation, where


The inspectors completed one sample.
vortexing of the shutdown cooling pumps may occur. To monitor reactor vessel water


====b. Findings====
level, operators used three RCS water level instruments when above 112 foot elevation.
No findings of significance were identified.
{{a|1R19}}
==1R19 Postmaintenance Testing (71111.19)==


====a. Inspection Scope====
The first level instrument was the wide-range reactor vessel refueling level instrument
The inspectors selected the nine below listed postmaintenance test activities of risk-significant systems or components. For each item, the inspectors:
: (1) reviewed the


applicable licensing basis and/or design basis documents to determine the safety
system (RVRLIS), which consisted of two pressure transmitters measuring the


functions;
differential pressure across the RCS. The reference leg transmitter was located at the
: (2) evaluated the safety functions that may have been affected by the


maintenance activity; and
top of the pressurizer and the variable leg transmitter was located at the Loop 4
: (3) reviewed the test procedure to ensure it adequately tested


the safety function that may have been affected. The inspectors either witnessed or
crossover leg. The second level instrument was LI-400, which is a clear standpipe with


reviewed test data to verify that acceptance criteria were met, plant impacts were
internal flags that indicate water level. LI-400 had essentially the same range and


evaluated, test equipment was calibrated, procedures were followed, jumpers were
instrument tap locations as wide-range RVRLIS. The third level instrument was the


properly controlled, the test data results were complete and accurate, the test equipment
narrow-range RVRLIS, which also consisted of two pressure transmitters that measured


was removed, the system was properly realigned, and deficiencies during testing were
the differential pressure across the upper portion of the reactor vessel. The reference


documented. The inspectors also reviewed the FSAR Update to determine if PG&E
leg transmitter was located at the reactor head vent, and the variable leg transmitter was


identified and corrected problems related to postmaintenance testing.
located at the Loop 3 hot leg.


-21-*April 18, 2006:  Unit 2, Containment Spray Pump 2-1 and 2-2*April 20, 2006:  Unit 2, Source Range Nuclear Instrument 31
On April 20, 2006, in preparation for reactor vessel head removal, operators lowered water level in the reactor vessel to the 112 foot elevation (2 feet below the vessel flange)
*May 2, 2006:  Unit 2, Component Cooling Water Pump 2-3
*May 2, 2006:  Unit 2, Vital Inverter IY-21
*May 2, 2006:  Unit 2, 4kV Vital Bus "H" Switchgear
*May 5, 2006:  Unit 2, Auxiliary Saltwater Pump 2-2
*May 11, 2006:  Unit 2, Centrifugal Charging Pump 2-1
*May 12, 2006:  Unit 2, Fuel transfer cart position resolver
*May 18, 2006:  Unit 2, Auxiliary Transformer 2-1 Documents reviewed by the inspectors are listed in the attachment.


The inspectors completed nine samples.
using Procedure OP A-2:II. At the 112 foot elevation, the time for water in the reactor


====b. Findings====
vessel to boil, if shutdown cooling were lost, was reduced to approximately 20 minutes.
No findings of significance were identified.
{{a|1R20}}
==1R20 Refueling and Outage Activities (71111.20)==


====a. Inspection Scope====
During the RCS draindown to the 112 foot elevation, Procedure OP A-2:II required
The inspectors reviewed the following risk-significant refueling items or outage activities to verify defense-in-depth commensurate with the outage risk control plan, compliance


with the TS, and adherence to commitments in response to Generic Letter 88-17, "Loss
operators to maintain wide-range RVRLIS and LI-400 level indications in agreement by


of Decay Heat Removal":
+/- 9 inches. However, Procedure OP A-2:II did not require the instruments to agree
: (1) the risk control plan;
: (2) tagging/clearance activities;
: (3) RCS instrumentation;
: (4) electrical power;
: (5) decay heat removal;
: (6) spent fuel pool


cooling;
once level reached the 112 foot elevation. Additionally, Procedure OP A-2:II allowed
: (7) inventory control;
: (8) reactivity control;
: (9) containment closure;
: (10) reduced


inventory or midloop conditions;
operators to place into service narrow-range RVRLIS and required it to read within
: (11) refueling activities;
: (12) heatup and cooldown


activities;
+/- 4 inches of LI-400 initially, but not for the duration of the RCS depressurization which
: (13) restart activities; and
: (14) identification and implementation of appropriate


corrective actions associated with refueling and outage activities. The inspectors'
was to follow.


containment inspections included observations of the containment sump for damage and
Once operators reached the 112 foot elevation and placed narrow-range RVRLIS in service, they began to depressurize the RCS according to Procedure OP A-2:II. During


debris and supports, braces, and snubbers for evidence of excessive stress, water
the depressurization, operators observed that both required instruments, wide-range


hammer, or aging. Documents reviewed by the inspectors included the Unit 2 Refueling
RVRLIS and LI-400 began to show increasing level, while the optional narrow-range


Outage 2R13 Outage Safety Plan.
RVRLIS water level remained stable at 112 feet. The deviation between narrow-range


The inspectors completed one sample.
RVRLIS and the other two instruments grew to approximately 15 inches before levels


====b. Findings====
stabilized. PG&E staff determined that a pressure differential existed between the gas
Introduction
:  An NRC-identified NCV of TS 5.4.1.a was determined for an inadequate procedure, Procedure OP A-2:II, "Reactor Vessel - Draining the RCS to the Vessel


Flange - With Fuel in Vessel," Revision 33A. Specifically, the procedure did not address
spaces of the pressurizer and reactor vessel. The RCS was depressurized via the


the reactor vessel level instrumentation required by the procedure deviated from actual
pressurizer relief tank with an approximate 1-inch outer diameter pipe. The


level by approximately 15 inches when the time to boiling in the reactor vessel was
communication path between the pressurizer and reactor vessel gas spaces was also an


approximately 20 minutes, if shutdown cooling were lost.
approximate 1-inch outer diameter pipe.


-22-Description
Despite the communication pathway, the depressurization activities would cause the pressurizer gas space to have a lower
:  One action to ensure the integrity of shutdown cooling by operators was to prevent reactor vessel water level from dropping below the 107.5 foot elevation, where


vortexing of the shutdown cooling pumps may occur. To monitor reactor vessel water
pressure than the reactor vessel gas space. Subsequently, the wide-range RVRLIS and


level, operators used three RCS water level instruments when above 112 foot elevation.
LI-400 instruments would read lower (reference from the pressurizer gas space) than


The first level instrument was the wide-range reactor vessel refueling level instrument
narrow-range RVRLIS (referenced from the reactor vessel gas space).


system (RVRLIS), which consisted of two pressure transmitters measuring the
The inspectors reviewed operating experience from both the Diablo Canyon Power Plant and the nuclear industry. Specifically, the inspectors reviewed Generic Letter 88-17, "Loss of Decay Heat Removal."  Generic Letter 88-17 specifically addressed reduced


differential pressure across the RCS. The reference leg transmitter was located at the
inventory evolutions, which is defined as 3 feet below the reactor vessel flange. While


top of the pressurizer and the variable leg transmitter was located at the Loop 4
the evolution on April 20, 2006, involved an RCS level that was only 2 feet below the  
-23-reactor vessel flange, the time-to-boiling estimate was short (approximately 20 minutes).


crossover leg. The second level instrument was LI-400, which is a clear standpipe with
Therefore, the inspectors determined that many of the recommendations in Generic


internal flags that indicate water level. LI-400 had essentially the same range and
Letter 88-17 could be considered as operating experience for this evolution. An example


instrument tap locations as wide-range RVRLIS. The third level instrument was the
of a recommendation was the consideration of various phenomena that could affect level


narrow-range RVRLIS, which also consisted of two pressure transmitters that measured
instrumentation, including the inability of gas spaces to communicate if the RCS legs are


the differential pressure across the upper portion of the reactor vessel. The reference
full of water. Also, Generic Letter 88-17 recommended reliable, accurate RCS water


leg transmitter was located at the reactor head vent, and the variable leg transmitter was
level information for operators whenever approaching or operating in a condition where a


located at the Loop 3 hot leg.
loss of level can lead to loss of decay heat removal. Through discussions with operators


On April 20, 2006, in preparation for reactor vessel head removal, operators lowered water level in the reactor vessel to the 112 foot elevation (2 feet below the vessel flange)
and a review of Procedure OP A-2:II, the inspectors observed that Diablo Canyon Power


using Procedure OP A-2:II. At the 112 foot elevation, the time for water in the reactor
Plant had operating experience that would demonstrate that the level instrumentation


vessel to boil, if shutdown cooling were lost, was reduced to approximately 20 minutes.
would tend to deviate when the RCS was being depressurzied.


During the RCS draindown to the 112 foot elevation, Procedure OP A-2:II required
The inspectors determined that PG&E staff had failed to adequately maintain Procedure OP A-2:II. First, wide-range RVRLIS and LI-400 were the required RCS level


operators to maintain wide-range RVRLIS and LI-400 level indications in agreement by
instruments during the RCS depressurization at the 112 foot elevation, even though


+/- 9 inches. However, Procedure OP A-2:II did not require the instruments to agree
these instruments would tend to read nonconservatively due to the pressure differences


once level reached the 112 foot elevation. Additionally, Procedure OP A-2:II allowed
in the gas spaces of the pressurizer and the reactor vessel. The inspectors determined


operators to place into service narrow-range RVRLIS and required it to read within
that an adequate review of operating experience would have demonstrated that these


+/- 4 inches of LI-400 initially, but not for the duration of the RCS depressurization which
level instruments were nonconservative for the depressurization evolution. Second, Procedure OP A-2:II did not have criteria regarding the performance of the RCS level


was to follow.
instruments during the RCS depressurization evolution. Although operators knew that


Once operators reached the 112 foot elevation and placed narrow-range RVRLIS in service, they began to depressurize the RCS according to Procedure OP A-2:II. During
RCS level instruments may deviate from each other during the depressurization, there


the depressurization, operators observed that both required instruments, wide-range
was no criteria that would have given operators information that abnormal level


RVRLIS and LI-400 began to show increasing level, while the optional narrow-range
deviations were occurring and may be indicative of unexpected equipment operation, problems, or phenomenon. Generic Letter 88-17 had recommended that licensees


RVRLIS water level remained stable at 112 feet. The deviation between narrow-range
consider various phenomenon that could affect level instrumentation and that reliable


RVRLIS and the other two instruments grew to approximately 15 inches before levels
and accurate RCS level information be provided to the operator to the extent possible


stabilized. PG&E staff determined that a pressure differential existed between the gas
when approaching conditions that could challenge loss of decay heat removal.


spaces of the pressurizer and reactor vessel. The RCS was depressurized via the
=====Analysis:=====
The performance deficiency associated with this finding involved the failure to maintain Procedure OP A-2:II. The finding is greater than minor because it is associated


pressurizer relief tank with an approximate 1-inch outer diameter pipe. The
with the Mitigating Systems Cornerstone attribute of procedure quality and affects the


communication path between the pressurizer and reactor vessel gas spaces was also an
associated cornerstone objective to ensure the availability, reliability, and capability of


approximate 1-inch outer diameter pipe.
systems that respond to initiating events to prevent undesirable consequences. Using


Despite the communication pathway, the depressurization activities would cause the pressurizer gas space to have a lower
IMC 0609, Appendix G, Attachment 1, Checklist 3, the finding is determined to be of very


pressure than the reactor vessel gas space. Subsequently, the wide-range RVRLIS and
low safety significance since one set of instrumentation provided accurate RCS level


LI-400 instruments would read lower (reference from the pressurizer gas space) than
indication and there was no loss of RCS inventory control. The finding had a crosscutting aspect in the area of human performance for resources because PG&E


narrow-range RVRLIS (referenced from the reactor vessel gas space).
failed to ensure the adequacy of the procedures used for reactor vessel level monitoring


The inspectors reviewed operating experience from both the Diablo Canyon Power Plant and the nuclear industry. Specifically, the inspectors reviewed Generic Letter 88-17, "Loss of Decay Heat Removal."  Generic Letter 88-17 specifically addressed reduced
to ensure nuclear safety.


inventory evolutions, which is defined as 3 feet below the reactor vessel flange. While
Enforcement
:  TS 5.4.1.a requires that written procedures be established, implemented, and maintained covering the activities specif ied in Appendix A, "Typical Procedures for Pressurized Water Reactors and Boiling Water Reactors," of Regulatory Guide 1.33, "Quality Assurance Program Requirements (Operation)," dated February 1978.


the evolution on April 20, 2006, involved an RCS level that was only 2 feet below the
Regulatory Guide 1.33, Appendix A, Section 2, requires procedures for refueling
-23-reactor vessel flange, the time-to-boiling estimate was short (approximately 20 minutes).


Therefore, the inspectors determined that many of the recommendations in Generic
operations. Contrary to this, Procedure OP A-2:II, "Reactor Vessel - Draining the RCS


Letter 88-17 could be considered as operating experience for this evolution. An example
to the Vessel Flange - With Fuel in Vessel," was inadequate because the procedures


of a recommendation was the consideration of various phenomena that could affect level
required the wide-range RVRLIS and LI-400 to be in service during RCS
-24-depressurization, despite operating experience that demonstrated these instruments would read nonconservatively. Additionally, Procedure OP A-2:II did not have criteria


instrumentation, including the inability of gas spaces to communicate if the RCS legs are
that alerted operators to abnormal level instrument deviations that may be caused by


full of water. Also, Generic Letter 88-17 recommended reliable, accurate RCS water
phenomena outside of the level deviations expected by the RCS depressurization.


level information for operators whenever approaching or operating in a condition where a
PG&E has planned to evaluate potential changes to Procedure OP A-2:II and RCS water


loss of level can lead to loss of decay heat removal. Through discussions with operators
level instrumentation when used during RCS depressurization. Because the finding is of


and a review of Procedure OP A-2:II, the inspectors observed that Diablo Canyon Power
very low safety significance and has been entered into PG&E's CAP as ARs A0664484, A0672419, and A0672422, this violation is being treated as an NCV consistent with


Plant had operating experience that would demonstrate that the level instrumentation
Section VI.A of the Enforcement Policy:  NCV 50-323/06-03-03, Inadequate Refueling


would tend to deviate when the RCS was being depressurzied.
Procedure for Draining and Depressurizing the Reactor Coolant System.
{{a|1R22}}
==1R22 Surveillance Testing (71111.22)==


The inspectors determined that PG&E staff had failed to adequately maintain Procedure OP A-2:II. First, wide-range RVRLIS and LI-400 were the required RCS level
====a. Inspection Scope====
The inspectors reviewed the FSAR Update, procedure requirements, and TS to ensure that the six below listed surveillance activities demonstrated that the SSC's tested were


instruments during the RCS depressurization at the 112 foot elevation, even though
capable of performing their intended safety functions. The inspectors either witnessed


these instruments would tend to read nonconservatively due to the pressure differences
or reviewed test data to verify that the following significant surveillance test attributes


in the gas spaces of the pressurizer and the reactor vessel. The inspectors determined
were adequate:
: (1) preconditioning;
: (2) evaluation of testing impact on the plant;
: (3) acceptance criteria;
: (4) test equipment;
: (5) procedures;
: (6) jumpers;
: (7) test data;
: (8) testing frequency and method demonstrated TS operability;
: (9) test equipment


that an adequate review of operating experience would have demonstrated that these
removal;
: (10) restoration of plant system s;
: (11) fulfillment of ASME Code requirements;
: (12) updating of performance indicator (PI) data;
: (13) engineering evaluations, root


level instruments were nonconservative for the depressurization evolution. Second, Procedure OP A-2:II did not have criteria regarding the performance of the RCS level
causes, and bases for returning tested SSCs not meeting the test acceptance criteria


instruments during the RCS depressurization evolution. Although operators knew that
were correct;
: (14) reference setting data; and
: (15) annunciators and alarm setpoints.


RCS level instruments may deviate from each other during the depressurization, there
The inspectors also verified that PG&E identified and implemented any needed


was no criteria that would have given operators information that abnormal level
corrective actions associated with the surveillance testing.*April 17, 2006:  Unit 1, Procedure STP M-9I, "Diesel Generator Start and Load Tracking," Revision 19, and STP M-9A, "Diesel Engine Generator Routine


deviations were occurring and may be indicative of unexpected equipment operation, problems, or phenomenon. Generic Letter 88-17 had recommended that licensees
Surveillance Test," Revision 70*April 19, 2006:  Unit 2, Procedures STP P-CSP-A22, "Comprehensive Testing of Containment Spray Pump 2-2," Revision 2 and STP P-CSP-A21, "Comprehensive Testing of Containment Spray Pump 2-1," Revision 1*May 1, 2006:  Unit 2, Procedure STP 102, "Test of Backup Nitrogen Accumulator System to Spray Valves and Charging Valves 8145, 8146, and 8147,"


consider various phenomenon that could affect level instrumentation and that reliable
Revision 23*May 8, 2006:  Unit 2, Procedure STP MP-I-7-T411H, "Control Bank D Rod Position Indication and Rod Stop C-11 Calibration," Revision 5A*May 8, 2006:  Units 1 and 2, Procedure SP-312, "Security System Emergency Power Source and Load Transferring System," Revision 15B*May 16, 2006:  Unit 2, Procedure STP 15, "Integrated Test of Engineered Safeguards and Diesel Generators," Revision 38A
-25-The inspectors completed six samples.


and accurate RCS level information be provided to the operator to the extent possible
====b. Findings====
No findings of significance were identified.


when approaching conditions that could challenge loss of decay heat removal.
===Cornerstone:  Emergency Preparedness1EP4Emergency Action Level and Emergency Plan Changes (71114.04)


=====Analysis:=====
====a. Inspection Scope====
The performance deficiency associated with this finding involved the failure to maintain Procedure OP A-2:II. The finding is greater than minor because it is associated
===


with the Mitigating Systems Cornerstone attribute of procedure quality and affects the
The inspectors performed in-office reviews of Revision 4, Change 5 to Section 4 of the Diablo Canyon, Units 1 and 2, Emergency Plan, and Revision 34 to Emergency Plan


associated cornerstone objective to ensure the availability, reliability, and capability of
Implementing Procedure EP G-1, "Emergency Classification and Emergency Plan


systems that respond to initiating events to prevent undesirable consequences. Using
Activation," both submitted in February 2006.


IMC 0609, Appendix G, Attachment 1, Checklist 3, the finding is determined to be of very
These revisions changed emergency classification level descriptions and revised emergency action levels as described in NRC Bulletin 2005-002, "Emergency


low safety significance since one set of instrumentation provided accurate RCS level
Preparedness and Response Actions for Security-Based Events." These revisions were compared to their previous revisions, to the criteria of NUREG-0654, "Criteria for Preparation and Evaluation of Radiological Emergency


indication and there was no loss of RCS inventory control. The finding had a crosscutting aspect in the area of human performance for resources because PG&E
Response Plans and Preparedness in Support of Nuclear Power Plants," Revision 1; to


failed to ensure the adequacy of the procedures used for reactor vessel level monitoring
Nuclear Energy Institute (NEI) 99-01, "Methodology for Development of Emergency Action Levels," Revision 2; to NRC Bulletin 2005-02, and to the requirements of


to ensure nuclear safety.
10 CFR 50.47(b) and 50.54(q), to determine if PG&E adequately implemented


Enforcement
10 CFR 50.54(q).
:  TS 5.4.1.a requires that written procedures be established, implemented, and maintained covering the activities specif ied in Appendix A, "Typical Procedures for Pressurized Water Reactors and Boiling Water Reactors," of Regulatory Guide 1.33, "Quality Assurance Program Requirements (Operation)," dated February 1978.


Regulatory Guide 1.33, Appendix A, Section 2, requires procedures for refueling
This review was not documented in a Safety Evaluation Report and did not constitute the approval of licensee changes; therefore, these changes are subject to future inspection.


operations. Contrary to this, Procedure OP A-2:II, "Reactor Vessel - Draining the RCS
The inspectors completed two samples during this inspection.


to the Vessel Flange - With Fuel in Vessel," was inadequate because the procedures
====b. Findings====
No findings of significance were identified.1EP6Emergency Preparedness Evaluation (71114.06)


required the wide-range RVRLIS and LI-400 to be in service during RCS
====a. Inspection Scope====
-24-depressurization, despite operating experience that demonstrated these instruments would read nonconservatively. Additionally, Procedure OP A-2:II did not have criteria
For drills contributing to drill/exercise performance and Emergency Response Organization PIs, the inspectors:
: (1) observed the training evolution to identify any


that alerted operators to abnormal level instrument deviations that may be caused by
weaknesses and deficiencies in classification, notification, and protective action


phenomena outside of the level deviations expected by the RCS depressurization.
recommendation development activities;
: (2) compared the identified weaknesses and


PG&E has planned to evaluate potential changes to Procedure OP A-2:II and RCS water
deficiencies against PG&E identified findings to determine whether PG&E is properly


level instrumentation when used during RCS depressurization. Because the finding is of
identifying failures; and
: (3) determined whether PG&E performance is in accordance
-26-with the guidance of the NEI 99-02, "Voluntary Submission of Performance Indicator Data," acceptance criteria.*June 1, 2006:  A full drill involving a main steam line break, a steam generator tube rupture, and failed fuel cladding, including the turnover between two
 
emergency response organization crews*June 9, 2006:  A simulator-based drill involving a main steam line break where a PI opportunity for classification of Notice of Unusual Event 28 existed Documents reviewed by the inspectors included the Diablo Canyon Power Plant Emergency Plan, Revision 4, and Lesson R061S5, "Imminent PTS," Revision 0.


very low safety significance and has been entered into PG&E's CAP as ARs A0664484, A0672419, and A0672422, this violation is being treated as an NCV consistent with
The inspectors completed two samples.


Section VI.A of the Enforcement Policy:  NCV 50-323/06-03-03, Inadequate Refueling
====b. Findings====
No findings of significance were identified.2.RADIATION SAFETY


Procedure for Draining and Depressurizing the Reactor Coolant System.
===Cornerstone:  Occupational Radiation Safety2OS1Access Control to Radiologically Significant Areas (71121.01)
{{a|1R22}}
==1R22 Surveillance Testing (71111.22)==


====a. Inspection Scope====
====a. Inspection Scope====
The inspectors reviewed the FSAR Update, procedure requirements, and TS to ensure that the six below listed surveillance activities demonstrated that the SSC's tested were
===


capable of performing their intended safety functions. The inspectors either witnessed
This area was inspected to assess PG&E's performance in implementing physical and administrative controls for airborne radioactivity areas, radiation areas, high radiation


or reviewed test data to verify that the following significant surveillance test attributes
areas, and worker adherence to these controls. The inspectors used the requirements


were adequate:
in 10 CFR Part 20, the TSs, and PG&E's procedures required by TSs as criteria for
: (1) preconditioning;
: (2) evaluation of testing impact on the plant;
: (3) acceptance criteria;
: (4) test equipment;
: (5) procedures;
: (6) jumpers;
: (7) test data;
: (8) testing frequency and method demonstrated TS operability;
: (9) test equipment


removal;
determining compliance. During the inspection, the inspectors interviewed the radiation
: (10) restoration of plant system s;
: (11) fulfillment of ASME Code requirements;
: (12) updating of performance indicator (PI) data;
: (13) engineering evaluations, root


causes, and bases for returning tested SSCs not meeting the test acceptance criteria
protection manager, radiation protection supervisors, and radiation workers. The


were correct;
inspectors performed independent radiation dose rate measurements and reviewed the
: (14) reference setting data; and
: (15) annunciators and alarm setpoints.


The inspectors also verified that PG&E identified and implemented any needed
following items:*PI events and associated documentation packages reported by PG&E in the Occupational Radiation Safety Cornerstone *Controls (surveys, posting, and barricades) of radiation, high radiation, and airborne radioactivity areas *Radiation work permits, procedures, engineering controls, and air sampler locations *Conformity of electronic personal dosimeter alarm setpoints with survey indications and plant policy, and workers' knowledge of required actions when


corrective actions associated with the surveillance testing.*April 17, 2006:  Unit 1, Procedure STP M-9I, "Diesel Generator Start and Load Tracking," Revision 19, and STP M-9A, "Diesel Engine Generator Routine
their electronic personnel dosimeter noticeably malfunctions or alarms
 
-27-*Barrier integrity and performance of engineering controls in airborne radioactivity areas*Physical and programmatic controls for highly activated or contaminated materials (nonfuel) stored within spent fuel and other storage pools*Self-assessments, audits, licensee event reports, and special reports related to the access control program since the last inspection *Corrective action documents related to access controls
Surveillance Test," Revision 70*April 19, 2006:  Unit 2, Procedures STP P-CSP-A22, "Comprehensive Testing of Containment Spray Pump 2-2," Revision 2 and STP P-CSP-A21, "Comprehensive Testing of Containment Spray Pump 2-1," Revision 1*May 1, 2006:  Unit 2, Procedure STP 102, "Test of Backup Nitrogen Accumulator System to Spray Valves and Charging Valves 8145, 8146, and 8147,"
*Radiation work permit briefings and worker instructions
 
*Adequacy of radiological controls such as required surveys, radiation protection job coverage, and contamination controls during job performance*Dosimetry placement in high radiation work areas with significant dose rate gradients*Changes in licensee procedural controls of high dose rate - high radiation areas and very high radiation areas*Controls for special areas that have the potential to become very high radiation areas during certain plant operations*Posting and locking of entrances to all accessible high dose rate - high radiation areas and very high radiation areas*Radiation worker and radiation protection technician performance with respect to radiation protection work requirements The inspectors completed 19 samples.
Revision 23*May 8, 2006:  Unit 2, Procedure STP MP-I-7-T411H, "Control Bank D Rod Position Indication and Rod Stop C-11 Calibration," Revision 5A*May 8, 2006:  Units 1 and 2, Procedure SP-312, "Security System Emergency Power Source and Load Transferring System," Revision 15B*May 16, 2006:  Unit 2, Procedure STP 15, "Integrated Test of Engineered Safeguards and Diesel Generators," Revision 38A
-25-The inspectors completed six samples.


====b. Findings====
====b. Findings====
No findings of significance were identified.
Introduction
:  The inspectors identified a noncited violation of 10 CFR 20.1501(a)because PG&E failed to perform a survey to identify the magnitude and extent of radiation levels for radiological hazards. The violation had very low safety significance.


===Cornerstone:===
Description
Emergency Preparedness1EP4Emergency Action Level and Emergency Plan Changes (71114.04)
: On April 18, 2006, the inspectors toured the 100-foot elevation of the Unit 2 auxiliary building and identified elevated radiat ion levels near Chemical Volume Control System Valves CVCS-2-8502 and CVCS-2
-8512A. Subsequent surveys by PG&E confirmed radiation levels of up to 200 millirem per hour on contact and 28 millirem per hour at 30 centimeters in this area. From a review of a previous survey map, the inspectors noted that the highest general area radiation level in the area was


====a. Inspection Scope====
approximately 5 millirem per hour. Unit 2 began a plant evolution (RCS forced oxygenation) that had the potential to raise radiation levels in several areas of the unit.
The inspectors performed in-office reviews of Revision 4, Change 5 to Section 4 of the Diablo Canyon, Units 1 and 2, Emergency Plan, and Revision 34 to Emergency Plan


Implementing Procedure EP G-1, "Emergency Classification and Emergency Plan
Due to the forced oxygenation process, PG&E implemented their posting guides and


Activation," both submitted in February 2006.
restricted personnel access to high radiation areas in Unit 2 that had potentially higher-
-28-than-normal radiation levels. However, PG&E did not restrict personnel access to radiation areas or survey a hallway on the 100-foot elevation that had the potential for higher-than-normal radiation levels prior to allowing personnel to enter them. PG&E's


These revisions changed emergency classification level descriptions and revised emergency action levels as described in NRC Bulletin 2005-002, "Emergency
posting guides did not address any actions that needed to be implemented for radiation


Preparedness and Response Actions for Security-Based Events." These revisions were compared to their previous revisions, to the criteria of NUREG-0654, "Criteria for Preparation and Evaluation of Radiological Emergency
areas or the hallways of the 100-foot elevation. The inspectors determined that PG&E


Response Plans and Preparedness in Support of Nuclear Power Plants," Revision 1; to
failed to survey the area to determine the magnitude and extent of the radiation levels


Nuclear Energy Institute (NEI) 99-01, "Methodology for Development of Emergency Action Levels," Revision 2; to NRC Bulletin 2005-02, and to the requirements of
and to evaluate the radiological hazards prior to allowing personnel to enter the area and


10 CFR 50.47(b) and 50.54(q), to determine if PG&E adequately implemented
whether the posting guides communicated any required action.


10 CFR 50.54(q).
=====Analysis:=====
The failure to survey is a performance deficiency. The finding was greater than minor because it was associated with the Occupational Radiation Safety


This review was not documented in a Safety Evaluation Report and did not constitute the approval of licensee changes; therefore, these changes are subject to future inspection.
Cornerstone attribute of Exposure Control and Monitoring and affected the cornerstone


The inspectors completed two samples during this inspection.
objective to ensure the adequate protection of a worker's health and safety from


====b. Findings====
exposure to radiation because workers could have unknowingly received additional
No findings of significance were identified.1EP6Emergency Preparedness Evaluation (71114.06)


====a. Inspection Scope====
radiation exposure from the increase in radiation levels. Because the finding involved
For drills contributing to drill/exercise performance and Emergency Response Organization PIs, the inspectors:
: (1) observed the training evolution to identify any


weaknesses and deficiencies in classification, notification, and protective action
the potential for unplanned, unintended dose resulting from conditions that were contrary


recommendation development activities;
to NRC regulations, the finding was evaluated using the Occupational Radiation Safety
: (2) compared the identified weaknesses and


deficiencies against PG&E identified findings to determine whether PG&E is properly
Significance Determination Process. The finding was determined to be of very low


identifying failures; and
safety significance because:
: (3) determined whether PG&E performance is in accordance
: (1) it did not involve as low as reasonably
-26-with the guidance of the NEI 99-02, "Voluntary Submission of Performance Indicator Data," acceptance criteria.*June 1, 2006:  A full drill involving a main steam line break, a steam generator tube rupture, and failed fuel cladding, including the turnover between two


emergency response organization crews*June 9, 2006: A simulator-based drill involving a main steam line break where a PI opportunity for classification of Notice of Unusual Event 28 existed Documents reviewed by the inspectors included the Diablo Canyon Power Plant Emergency Plan, Revision 4, and Lesson R061S5, "Imminent PTS," Revision 0.
achievable (ALARA) planning or work controls,
: (2) there was no personnel


The inspectors completed two samples.
overexposure,
: (3) there was no substantial potential for personnel overexposure, and
: (4) the finding did not compromise PG&E's ability to assess dose. The finding had


====b. Findings====
crosscutting aspects associated with human performance because adequate resources
No findings of significance were identified.2.RADIATION SAFETY


===Cornerstone:===
were not established for the survey requirements.
Occupational Radiation Safety2OS1Access Control to Radiologically Significant Areas (71121.01)


====a. Inspection Scope====
Enforcement
This area was inspected to assess PG&E's performance in implementing physical and administrative controls for airborne radioactivity areas, radiation areas, high radiation
:  10 CFR 20.1501(a) requires that each licensee make or cause to be made surveys that may be necessary to comply with the regulations in Part 20 to


areas, and worker adherence to these controls. The inspectors used the requirements
determine the extent and magnitude of radiation levels and to evaluate the radiological


in 10 CFR Part 20, the TSs, and PG&E's procedures required by TSs as criteria for
hazards. Pursuant to 10 CFR 20.1003, survey means an evaluation of the radiological


determining compliance. During the inspection, the inspectors interviewed the radiation
conditions and potential hazards incident to the production, use, transfer, release, disposal, or presence of radioactive material or other sources of radiation. Contrary to


protection manager, radiation protection supervisors, and radiation workers. The
this requirement, on April 18, 2006, PG&E failed to survey the 100-foot elevation of the


inspectors performed independent radiation dose rate measurements and reviewed the
Unit 2 auxiliary building to assure compliance with 10 CFR 20.1201, which limits


following items:*PI events and associated documentation packages reported by PG&E in the Occupational Radiation Safety Cornerstone *Controls (surveys, posting, and barricades) of radiation, high radiation, and airborne radioactivity areas *Radiation work permits, procedures, engineering controls, and air sampler locations *Conformity of electronic personal dosimeter alarm setpoints with survey indications and plant policy, and workers' knowledge of required actions when
radiation exposure to occupational workers to 5.0 rem total effective dose equivalent.


their electronic personnel dosimeter noticeably malfunctions or alarms
This violation was entered into PG&E's CAP as AR 0665039. Because this finding is of
-27-*Barrier integrity and performance of engineering controls in airborne radioactivity areas*Physical and programmatic controls for highly activated or contaminated materials (nonfuel) stored within spent fuel and other storage pools*Self-assessments, audits, licensee event reports, and special reports related to the access control program since the last inspection *Corrective action documents related to access controls
*Radiation work permit briefings and worker instructions
*Adequacy of radiological controls such as required surveys, radiation protection job coverage, and contamination controls during job performance*Dosimetry placement in high radiation work areas with significant dose rate gradients*Changes in licensee procedural controls of high dose rate - high radiation areas and very high radiation areas*Controls for special areas that have the potential to become very high radiation areas during certain plant operations*Posting and locking of entrances to all accessible high dose rate - high radiation areas and very high radiation areas*Radiation worker and radiation protection technician performance with respect to radiation protection work requirements The inspectors completed 19 samples.


====b. Findings====
very low safety significance and was entered into PG&E's CAP, it is being treated as an
Introduction
:  The inspectors identified a noncited violation of 10 CFR 20.1501(a)because PG&E failed to perform a survey to identify the magnitude and extent of radiation levels for radiological hazards. The violation had very low safety significance.


Description
NCV, consistent with Section VI.A.1 of the NRC Enforcement Policy:
:  On April 18, 2006, the inspectors toured the 100-foot elevation of the Unit 2 auxiliary building and identified elevated radiat ion levels near Chemical Volume Control System Valves CVCS-2-8502 and CVCS-2
-8512A. Subsequent surveys by PG&E confirmed radiation levels of up to 200 millirem per hour on contact and 28 millirem per hour at 30 centimeters in this area. From a review of a previous survey map, the inspectors noted that the highest general area radiation level in the area was


approximately 5 millirem per hour. Unit 2 began a plant evolution (RCS forced oxygenation) that had the potential to raise radiation levels in several areas of the unit.
NCV 50-323/06-03-04, Failure to Survey to Identify the Magnitude and Extent of


Due to the forced oxygenation process, PG&E implemented their posting guides and
Radiation Levels to Identify Radiological Hazards.2OS2ALARA Planning and Controls (71121.02)


restricted personnel access to high radiation areas in Unit 2 that had potentially higher-
====a. Inspection Scope====
-28-than-normal radiation levels. However, PG&E did not restrict personnel access to radiation areas or survey a hallway on the 100-foot elevation that had the potential for higher-than-normal radiation levels prior to allowing personnel to enter them. PG&E's
The inspectors assessed PG&E's performance with respect to maintaining individual and collective radiation exposures ALARA. The inspectors used the requirements in 10 CFR


posting guides did not address any actions that needed to be implemented for radiation
Part 20 and PG&E's procedures required by TS as criteria for determining compliance.


areas or the hallways of the 100-foot elevation. The inspectors determined that PG&E
The inspectors interviewed PG&E personnel and reviewed:
-29-*Five (to 10) outage or on-line maintenance work activities scheduled during the inspection period and associated work activity exposure estimates which were


failed to survey the area to determine the magnitude and extent of the radiation levels
likely to result in the highest personnel collective exposures *ALARA work activity evaluations, exposure estimates, and exposure mitigation requirements *Integration of ALARA requirements into work procedure and radiation work permit documents *Person-hour estimates provided by maintenance planning and other groups to the radiation protection group with the actual work activity time requirements *Dose rate reduction activities in work planning
*Workers use of the low dose waiting areas
*First-line job supervisors' contribution to ensuring work activities are conducted in a dose efficient manner*Radiation worker and radiation protection technician performance during work activities in radiation areas, airborne radioactivity areas, or high radiation areas *Self-assessments, audits, and special reports related to the ALARA program since the last inspection The inspectors completed nine samples.


and to evaluate the radiological hazards prior to allowing personnel to enter the area and
====b. Findings====
No findings of significance were identified.4.


whether the posting guides communicated any required action.
==OTHER ACTIVITIES==
{{a|4OA1}}
==4OA1 PI Verification==
{{IP sample|IP=IP 71151}}
===.1 Cornerstone:===
Occupational Radiation Safety*Occupational Exposure Control Effectiveness


=====Analysis:=====
====a. Inspection Scope====
The failure to survey is a performance deficiency. The finding was greater than minor because it was associated with the Occupational Radiation Safety
The inspectors reviewed PG&E's documents from January 1 through March 31, 2006.


Cornerstone attribute of Exposure Control and Monitoring and affected the cornerstone
The review included corrective action documentation that identified occurrences in


objective to ensure the adequate protection of a worker's health and safety from
locked high radiation areas (as defined in PG&E's TS), very high radiation areas (as


exposure to radiation because workers could have unknowingly received additional
defined in 10 CFR 20.003), and unplanned personnel exposures (as defined in


radiation exposure from the increase in radiation levels. Because the finding involved
NEI 99-02). Additional records reviewed included ALARA records and whole body


the potential for unplanned, unintended dose resulting from conditions that were contrary
counts of selected individual exposures. The inspectors interviewed PG&E personnel


to NRC regulations, the finding was evaluated using the Occupational Radiation Safety
who were accountable for collecting and evaluating the PI data. In addition, the
-30-inspectors toured plant areas to verify that high radiation, locked high radiation, and very high radiation areas were properly controlled. PI definitions and guidance contained in


Significance Determination Process. The finding was determined to be of very low
NEI 99-02, "Regulatory Assessment Indicator Guideline," Revision 3, were used to verify


safety significance because:
the basis in reporting for each data element.
: (1) it did not involve as low as reasonably


achievable (ALARA) planning or work controls,
The inspectors completed one sample in this cornerstone.
: (2) there was no personnel


overexposure,
====b. Findings====
: (3) there was no substantial potential for personnel overexposure, and
No findings of significance were identified.
: (4) the finding did not compromise PG&E's ability to assess dose. The finding had


crosscutting aspects associated with human performance because adequate resources
===.2 Cornerstone:===
Public Radiation Safety*Radiological Effluent Technical Specification/Offsite Dose Calculation Manual Radiological Effluent Occurrences


were not established for the survey requirements.
====a. Inspection Scope====
The inspectors reviewed PG&E's documents from January 1 through March 31, 2006.


Enforcement
PG&E's records reviewed included corrective action documentation that identified
:  10 CFR 20.1501(a) requires that each licensee make or cause to be made surveys that may be necessary to comply with the regulations in Part 20 to


determine the extent and magnitude of radiation levels and to evaluate the radiological
occurrences for liquid or gaseous effluent releases that exceeded PI thresholds and


hazards. Pursuant to 10 CFR 20.1003, survey means an evaluation of the radiological
those reported to the NRC. The inspectors interviewed PG&E personnel who were


conditions and potential hazards incident to the production, use, transfer, release, disposal, or presence of radioactive material or other sources of radiation. Contrary to
accountable for collecting and evaluating the PI data. PI definitions and guidance


this requirement, on April 18, 2006, PG&E failed to survey the 100-foot elevation of the
contained in NEI 99-02, "Regulatory Assessment Indicator Guideline," Revision 3, were


Unit 2 auxiliary building to assure compliance with 10 CFR 20.1201, which limits
used to verify the basis in reporting for each data element.


radiation exposure to occupational workers to 5.0 rem total effective dose equivalent.
The inspectors completed one sample in this cornerstone.


This violation was entered into PG&E's CAP as AR 0665039. Because this finding is of
====b. Findings====
No findings of significance were identified.4OA2Identification and Resolution of Problems (71152)


very low safety significance and was entered into PG&E's CAP, it is being treated as an
===.1 Routine Review of Identification and Resolution of Problems===


NCV, consistent with Section VI.A.1 of the NRC Enforcement Policy:
====a. Inspection Scope====
The inspectors performed a daily screening of items entered into PG&E's CAP. This assessment was accomplished by reviewing ARs and event trend reports and attending


NCV 50-323/06-03-04, Failure to Survey to Identify the Magnitude and Extent of
daily operational meetings. The inspectors:
: (1) verified that equipment, human


Radiation Levels to Identify Radiological Hazards.2OS2ALARA Planning and Controls (71121.02)
performance, and program issues were being identified by PG&E at an appropriate


====a. Inspection Scope====
threshold and that the issues were entered into the CAP;
The inspectors assessed PG&E's performance with respect to maintaining individual and collective radiation exposures ALARA. The inspectors used the requirements in 10 CFR
: (2) verified that corrective


Part 20 and PG&E's procedures required by TS as criteria for determining compliance.
actions were commensurate with the significance of the issue; and
: (3) identified
 
conditions that might warrant additional follow-up through other baseline inspection


The inspectors interviewed PG&E personnel and reviewed:
procedures.
-29-*Five (to 10) outage or on-line maintenance work activities scheduled during the inspection period and associated work activity exposure estimates which were


likely to result in the highest personnel collective exposures *ALARA work activity evaluations, exposure estimates, and exposure mitigation requirements *Integration of ALARA requirements into work procedure and radiation work permit documents *Person-hour estimates provided by maintenance planning and other groups to the radiation protection group with the actual work activity time requirements *Dose rate reduction activities in work planning
-31-
*Workers use of the low dose waiting areas
*First-line job supervisors' contribution to ensuring work activities are conducted in a dose efficient manner*Radiation worker and radiation protection technician performance during work activities in radiation areas, airborne radioactivity areas, or high radiation areas *Self-assessments, audits, and special reports related to the ALARA program since the last inspection The inspectors completed nine samples.


====b. Findings====
====b. Findings====
No findings of significance were identified.4.
No findings of significance were identified.


==OTHER ACTIVITIES==
===.2 Selected Issue Follow-Up Inspection===
{{a|4OA1}}
==4OA1 PI Verification==
{{IP sample|IP=IP 71151}}
===.1 Cornerstone:===
Occupational Radiation Safety*Occupational Exposure Control Effectiveness


====a. Inspection Scope====
====a. Inspection Scope====
The inspectors reviewed PG&E's documents from January 1 through March 31, 2006.
In addition to the routine review, the inspectors selected the one below listed issue for a more in-depth review. The inspectors considered the following during the review of


The review included corrective action documentation that identified occurrences in
PG&E's actions:
: (1) complete and accurate identification of the problem in a timely


locked high radiation areas (as defined in PG&E's TS), very high radiation areas (as
manner;
: (2) evaluation and disposition of operability/reportability issues;
: (3) consideration of extent of condition, generic implications, common cause, and


defined in 10 CFR 20.003), and unplanned personnel exposures (as defined in
previous occurrences;
: (4) classification and prioritization of the resolution of the problem;
: (5) identification of root and contributing causes of the problem;
: (6) identification of


NEI 99-02). Additional records reviewed included ALARA records and whole body
corrective actions; and
 
: (7) completion of corrective actions in a timely manner.*April 26, 2006:  High Stator Temperature Trends on Component Cooling Water Motors Documents reviewed by the inspectors are listed in the attachment.
counts of selected individual exposures. The inspectors interviewed PG&E personnel
 
who were accountable for collecting and evaluating the PI data. In addition, the  
-30-inspectors toured plant areas to verify that high radiation, locked high radiation, and very high radiation areas were properly controlled. PI definitions and guidance contained in
 
NEI 99-02, "Regulatory Assessment Indicator Guideline," Revision 3, were used to verify
 
the basis in reporting for each data element.
 
The inspectors completed one sample in this cornerstone.


====b. Findings====
====b. Findings====
No findings of significance were identified.
No findings of significance were identified.


===.2 Cornerstone:===
===.3 Semiannual Trend Review===
Public Radiation Safety*Radiological Effluent Technical Specification/Offsite Dose Calculation Manual Radiological Effluent Occurrences


====a. Inspection Scope====
====a. Inspection Scope====
The inspectors reviewed PG&E's documents from January 1 through March 31, 2006.
The inspectors completed a semiannual trend review of repetitive or closely-related issues that were documented in ARs, system and component health reports, quality


PG&E's records reviewed included corrective action documentation that identified
assurance audits, trend reports, Diablo Canyon internal PIs, and NRC inspection reports


occurrences for liquid or gaseous effluent releases that exceeded PI thresholds and
to identify trends that might indicate the existence of more safety-significant issues. The


those reported to the NRC. The inspectors interviewed PG&E personnel who were
inspectors' review consisted of the 6-month period of January 1 to June 30, 2006. When


accountable for collecting and evaluating the PI data. PI definitions and guidance
warranted, some of the samples expanded beyond those dates to fully assess the issue.
 
The inspectors also reviewed CAP items associated with troubleshooting. The
 
inspectors compared and contrasted their results with the results contained in PG&E's


contained in NEI 99-02, "Regulatory Assessment Indicator Guideline," Revision 3, were
quarterly trend reports. Corrective actions associated with a sample of the issues


used to verify the basis in reporting for each data element.
identified in PG&E's trend report were reviewed for adequacy. Documents reviewed by


The inspectors completed one sample in this cornerstone.
the inspectors are listed in the attachment.


====b. Findings====
====b. Findings====
No findings of significance were identified.4OA2Identification and Resolution of Problems (71152)
The inspectors reviewed Quality Verification Assessment 060480001, "Troubleshooting,"
dated April 14, 2006. The purpose of the assessment was to evaluate the


===.1 Routine Review of Identification and Resolution of Problems===
implementation of the troubleshooting program as described in Procedure MA1.DC10, "Troubleshooting," Revision 9. Quality Verification identified a need for improvement in


====a. Inspection Scope====
documentation of problem statements, data acquisition results, determination of possible
The inspectors performed a daily screening of items entered into PG&E's CAP. This assessment was accomplished by reviewing ARs and event trend reports and attending
-32-failure modes, troubleshooting plans, and analysis of results. In particular, maintenance personnel's implementation of the troubleshooting procedure often did not meet the


daily operational meetings. The inspectors:
troubleshooting attributes, while engineering personnel's implementation of
: (1) verified that equipment, human


performance, and program issues were being identified by PG&E at an appropriate
troubleshooting had only minor inconsistencies. Furthermore, the assessment observed


threshold and that the issues were entered into the CAP;
the need for improvement in the knowledge of troubleshooting requirements throughout
: (2) verified that corrective


actions were commensurate with the significance of the issue; and
the organization for:
: (3) identified
: (1) when troubleshooting should be implemented,
: (2) what types of


conditions that might warrant additional follow-up through other baseline inspection
equipment problems require troubleshooting, and
: (3) the level of planning and


procedures.
documentation required for low level equipment problems. Quality verification found that


-31-
Procedure MA1.DC10 continued to be difficult to use despite revisions to the procedure.


====b. Findings====
The inspectors also reviewed previous Quality Verification assessments, dating back to 2004, for troubleshooting observations. These assessments are listed in the
No findings of significance were identified.


===.2 Selected Issue Follow-Up Inspection===
attachment. While the assessments pointed out that the site has shown improvement in troubleshooting efforts since 2003, the inspectors observed that Quality Verification had


====a. Inspection Scope====
previously identified similar issues as those discussed above. The following are some
In addition to the routine review, the inspectors selected the one below listed issue for a more in-depth review. The inspectors considered the following during the review of


PG&E's actions:
insights from previous assessments, which also covered previous revisions to
: (1) complete and accurate identification of the problem in a timely


manner;
Procedure MA1.DC10.*In some instances, initial troubleshooting efforts failed to identify the cause of the problem for safety-related and/or risk-significant equipment.*On several occasions, the site was reluctant to enter a more rigorous/formal troubleshooting format, since it was seen as time consuming and the technicians
: (2) evaluation and disposition of operability/reportability issues;
: (3) consideration of extent of condition, generic implications, common cause, and


previous occurrences;
felt they knew better on how to approach the problem as opposed to following
: (4) classification and prioritization of the resolution of the problem;
: (5) identification of root and contributing causes of the problem;
: (6) identification of


corrective actions; and
Procedure MA1.DC10. As a result, there were instances where the cause
: (7) completion of corrective actions in a timely manner.*April 26, 2006:  High Stator Temperature Trends on Component Cooling Water Motors Documents reviewed by the inspectors are listed in the attachment.


====b. Findings====
determination was inaccurate, such as the case with Containment Spray
No findings of significance were identified.


===.3 Semiannual Trend Review===
Pump 2-2 control cable ground.*Procedure MA1.DC10 was deficient, making it difficult for maintenance personnel to comply with its requirements. Subsequently, personnel performing


====a. Inspection Scope====
troubleshooting relied upon their knowledge and experience to the exclusion of
The inspectors completed a semiannual trend review of repetitive or closely-related issues that were documented in ARs, system and component health reports, quality


assurance audits, trend reports, Diablo Canyon internal PIs, and NRC inspection reports
the requirements in the troubleshooting procedure.*In some instances, maintenance and engineering personnel were reluctant to characterize work activities as "troubleshooting" when in fact the activities


to identify trends that might indicate the existence of more safety-significant issues. The
involved the investigation of plant equipment problems. Quality Verification


inspectors' review consisted of the 6-month period of January 1 to June 30, 2006. When
recommended that senior management emphasize the expectations for


warranted, some of the samples expanded beyond those dates to fully assess the issue.
implementing Procedure MA1.DC10 when the criteria for entering the procedure


The inspectors also reviewed CAP items associated with troubleshooting. The
were met.*Quality Verification noted that the level of detail in troubleshooting documentation was weak. For example, as-found conditions were not documented, results of a


inspectors compared and contrasted their results with the results contained in PG&E's
component history search were not documented, and documentation of work


quarterly trend reports. Corrective actions associated with a sample of the issues
performed was not detailed.


identified in PG&E's trend report were reviewed for adequacy. Documents reviewed by
The inspectors have observed several troubleshooting activities that have occurred on site and, in general, agree with the assessments identified by Quality Verification. Most


the inspectors are listed in the attachment.
recently, the inspectors observed troubleshooting for AFW Discharge


====b. Findings====
Valves FW-1-LCV-107 and FW-1-LCV-108, as described in Section
The inspectors reviewed Quality Verification Assessment 060480001, "Troubleshooting,"
{{a|4OA5}}
dated April 14, 2006. The purpose of the assessment was to evaluate the
==4OA5 of this report.==


implementation of the troubleshooting program as described in Procedure MA1.DC10, "Troubleshooting," Revision 9. Quality Verification identified a need for improvement in
-33-The inspectors observed that troubleshooting for Valve FW-1-LCV-107 was performed by maintenance personnel. In reviewing the documentation from that troubleshooting


documentation of problem statements, data acquisition results, determination of possible  
effort, the inspectors could not identify any other possible failure mechanisms that had
-32-failure modes, troubleshooting plans, and analysis of results. In particular, maintenance personnel's implementation of the troubleshooting procedure often did not meet the


troubleshooting attributes, while engineering personnel's implementation of
been considered by Maintenance personnel other than the determined cause.


troubleshooting had only minor inconsistencies. Furthermore, the assessment observed
Additionally, the inspectors observed data that would tend to contradict the determined


the need for improvement in the knowledge of troubleshooting requirements throughout
cause of the valve, as described in Section 4OA5. The inspectors also observed


the organization for:
troubleshooting for Valve FW-1-LCV-108, which had similar indications as Valve
: (1) when troubleshooting should be implemented,
: (2) what types of


equipment problems require troubleshooting, and
FW-1-LCV-107 when it failed to stroke. The troubleshooting team consisted of both
: (3) the level of planning and


documentation required for low level equipment problems. Quality verification found that
Engineering and Maintenance personnel. The inspectors observed that the Engineering


Procedure MA1.DC10 continued to be difficult to use despite revisions to the procedure.
personnel were careful to:
: (1) preserve evidence by arranging the various investigative


The inspectors also reviewed previous Quality Verification assessments, dating back to 2004, for troubleshooting observations. These assessments are listed in the
activities,
: (2) consider various potential failu re mechanisms before investigative activities began, and
: (3) consider all data available to them. In summary, the inspectors felt that


attachment. While the assessments pointed out that the site has shown improvement in troubleshooting efforts since 2003, the inspectors observed that Quality Verification had
the observations made during the troubleshooting on Valves FW-1-LCV-107


previously identified similar issues as those discussed above. The following are some
and FW-1-LCV-108 confirmed the observations documented by Quality Verification in their assessments.


insights from previous assessments, which also covered previous revisions to
===.4 Occupational Radiation Safety===


Procedure MA1.DC10.*In some instances, initial troubleshooting efforts failed to identify the cause of the problem for safety-related and/or risk-significant equipment.*On several occasions, the site was reluctant to enter a more rigorous/formal troubleshooting format, since it was seen as time consuming and the technicians
====a. Inspection Scope====
The inspectors evaluated the effectiveness of PG&E's problem identification and resolution process with respect to the following inspection areas:*Access Control to Radiologically Significant Areas (Section 2OS1)*ALARA Planning and Controls (Section 2OS2)


felt they knew better on how to approach the problem as opposed to following
====b. Findings====
No findings of significance were identified.


Procedure MA1.DC10. As a result, there were instances where the cause
===.5 Inservice Inspection===


determination was inaccurate, such as the case with Containment Spray
====a. Inspection Scope====
The inspector reviewed the related condition reports on an inservice inspection issued during the current and past refueling outages and verified that PG&E identified, evaluated, corrected, and trended problems. The inspector evaluated the effectiveness


Pump 2-2 control cable ground.*Procedure MA1.DC10 was deficient, making it difficult for maintenance personnel to comply with its requirements. Subsequently, personnel performing
of PG&E's CAP, including the adequacy of the technical resolutions.


troubleshooting relied upon their knowledge and experience to the exclusion of
====b. Findings====
No findings of significance were identified.


the requirements in the troubleshooting procedure.*In some instances, maintenance and engineering personnel were reluctant to characterize work activities as "troubleshooting" when in fact the activities
-34-4OA3Event Followup (71153)


involved the investigation of plant equipment problems. Quality Verification
===.1 Main Turbine Trip Due to Personnel Error===


recommended that senior management emphasize the expectations for
====a. Inspection Scope====
On June 7, 2006, the inspector reviewed the actions taken prior to, during, and following a main turbine trip on Unit 2, on May 25, 2006. Operations personnel were attempting to


implementing Procedure MA1.DC10 when the criteria for entering the procedure
parallel the main generator to the grid during the reactor startup, following a refueling


were met.*Quality Verification noted that the level of detail in troubleshooting documentation was weak. For example, as-found conditions were not documented, results of a
outage.


component history search were not documented, and documentation of work
====b. Findings====
No findings of significance were identified.


performed was not detailed.
===.2 (Closed) Licensee Event Report 50-275/1-2005-001-00 Steam Generator Tube Plugging===


The inspectors have observed several troubleshooting activities that have occurred on site and, in general, agree with the assessments identified by Quality Verification. Most
Because of Stress Corrosion Cracking On November 11, 2005, PG&E determined that analysis of eddy current testing on Steam Generators 1-1 and 1-2 indicated that greater than one percent of the tubes were


recently, the inspectors observed troubleshooting for AFW Discharge
defective as a result of outside diameter stress corrosion cracking at the hot leg tube


Valves FW-1-LCV-107 and FW-1-LCV-108, as described in Section
support plates and at the hot leg top of tubesheet. This determination occurred at the
{{a|4OA5}}
==4OA5 of this report.==


-33-The inspectors observed that troubleshooting for Valve FW-1-LCV-107 was performed by maintenance personnel. In reviewing the documentation from that troubleshooting
end of Operating Cycle 13. The inspector verified that PG&E took effective corrective


effort, the inspectors could not identify any other possible failure mechanisms that had
action. All defective tubes were plugged and removed from service in accordance with


been considered by Maintenance personnel other than the determined cause.
TS 5.5.9, "Steam Generator (SG) Tube Surveillance Program."  The licensing basis accident analysis assumes a tube plugging limit of 15 percent per steam generator. The


Additionally, the inspectors observed data that would tend to contradict the determined
plugging percentage for each Unit 1 steam generator remains within the current


cause of the valve, as described in Section 4OA5. The inspectors also observed
allowable limit of 15 percent. Steam Generator 1-1 has 6.8 percent plugged and Steam


troubleshooting for Valve FW-1-LCV-108, which had similar indications as Valve
Generator 1-2 has 9.3 percent plugged. PG&E maintains a comprehensive program to


FW-1-LCV-107 when it failed to stroke. The troubleshooting team consisted of both
minimize steam generator tube degradation and plans to replace the steam generators


Engineering and Maintenance personnel. The inspectors observed that the Engineering
at the end of Operating Cycle 15. This licensee event report is closed.


personnel were careful to:
4OA5Other
: (1) preserve evidence by arranging the various investigative


activities,
===.1 TI 2515/160 - Pressurizer Penetration Nozzles and Steam Space Piping Connections in===
: (2) consider various potential failu re mechanisms before investigative activities began, and
: (3) consider all data available to them. In summary, the inspectors felt that


the observations made during the troubleshooting on Valves FW-1-LCV-107
U.S. Pressurized Water Reactors


and FW-1-LCV-108 confirmed the observations documented by Quality Verification in their assessments.
====a. Inspection Scope====
The inspectors reviewed PG&E's actions regarding the inspection and repair associated with Alloy 82/182/600 material that may have been used in pressurizer penetration


===.4 Occupational Radiation Safety===
nozzles, steam space piping connections, heads, and shells. Specifically, the inspectors


====a. Inspection Scope====
reviewed PG&E's response to NRC Bulletin 2004-01, "Inspection of Alloy 82/182/600
The inspectors evaluated the effectiveness of PG&E's problem identification and resolution process with respect to the following inspection areas:*Access Control to Radiologically Significant Areas (Section 2OS1)*ALARA Planning and Controls (Section 2OS2)


====b. Findings====
Materials Used in the Fabrication of Pressurizer Penetrations and Steam Space Piping
No findings of significance were identified.


===.5 Inservice Inspection===
Connections at Pressurized Water Reactors."  PG&E documented in their response to


====a. Inspection Scope====
the bulletin that the Unit 2 pressurizer utilized Alloy 82/182 material in the nozzle to safe
The inspector reviewed the related condition reports on an inservice inspection issued during the current and past refueling outages and verified that PG&E identified, evaluated, corrected, and trended problems. The inspector evaluated the effectiveness


of PG&E's CAP, including the adequacy of the technical resolutions.
end welds for the surge line, the pressurizer safety lines, the power-operated relief valve
-35-lines, and the spray line. Stainless steel was used in all other pressurizer penetration welds. In PG&E's response to the bulletin, they committed to a bare metal visual exam
 
of all the welds that had Alloy 82/182 material.
 
The inspectors reviewed PG&E's response to NRC Bulletin 2004-01 and observed their inspection activities for the Unit 2 pressurizer. The inspectors verified the qualifications


====b. Findings====
of personnel performing the bare metal exam and independently observed several of the
No findings of significance were identified.


-34-4OA3Event Followup (71153)
subject pressurizer penetration welds for evidence of boric acid deposits and the


===.1 Main Turbine Trip Due to Personnel Error===
capability to perform the bare metal exam. The inspectors reviewed Procedure ISI VT 2-1, "Visual Examination During Section XI System Pressure Test,"


====a. Inspection Scope====
Revision 0, during the inspection.
On June 7, 2006, the inspector reviewed the actions taken prior to, during, and following a main turbine trip on Unit 2, on May 25, 2006. Operations personnel were attempting to


parallel the main generator to the grid during the reactor startup, following a refueling
The activities required in Temporary Instruction (TI) 2515/160 for Diablo Canyon Power Plant Unit 2 have been completed. Documents reviewed by the inspectors are listed in


outage.
the attachment. This TI is closed for Unit 2.


====b. Findings====
====b. Findings====
No findings of significance were identified.
No findings of significance were identified.


===.2 (Closed) Licensee Event Report 50-275/1-2005-001-00 Steam Generator Tube Plugging===
===.2 TI 2515/165 - Operational Readiness of Offsite Power and Impact on Plant Risk===


Because of Stress Corrosion Cracking On November 11, 2005, PG&E determined that analysis of eddy current testing on Steam Generators 1-1 and 1-2 indicated that greater than one percent of the tubes were
====a. Inspection Scope====
The objective of TI 2515/165, "Operational Readiness of Offsite Power and Impact on Plant Risk," is to gather information to support the assessment of nuclear power plant


defective as a result of outside diameter stress corrosion cracking at the hot leg tube
operational readiness of offsite power systems and impact on plant risk. During this


support plates and at the hot leg top of tubesheet. This determination occurred at the
inspection, the inspectors interviewed PG&E personnel, reviewed applicable procedures, and gathered information for further evaluation by the Office of Nuclear Reactor


end of Operating Cycle 13. The inspector verified that PG&E took effective corrective
Regulation.


action. All defective tubes were plugged and removed from service in accordance with
====b. Findings====
No findings of significance were identified.


TS 5.5.9, "Steam Generator (SG) Tube Surveillance Program."  The licensing basis accident analysis assumes a tube plugging limit of 15 percent per steam generator. The
===.3 (Closed) Unresolved Item (URI) 05000275/05-05-03:===
Corrective Actions to Prevent Repetitive Failures of AFW Limitorque Valves


plugging percentage for each Unit 1 steam generator remains within the current
====a. Inspection Scope====
The inspectors performed additional inspection associated with this URI to determine any performance issues associated with design and maintenance practices regarding


allowable limit of 15 percent. Steam Generator 1-1 has 6.8 percent plugged and Steam
Limitorque actuators. The inspectors also evaluated any extent of condition and/or


Generator 1-2 has 9.3 percent plugged. PG&E maintains a comprehensive program to
generic impacts.


minimize steam generator tube degradation and plans to replace the steam generators
====b. Findings====
Introduction
:  A Green, NRC-identified NCV was identified for the failure to correct a significant condition adverse to quality as required by 10 CFR Part 50, Appendix B,
-36-Criterion XVI, "Corrective Action."  Specifically, PG&E failed to preclude repetition of similar failures with Limitorque Model SMB-000 motor-operated valves in the AFW


at the end of Operating Cycle 15. This licensee event report is closed.
system. The failure of these motor-operated valves affected the ability of the valves to


4OA5Other
be operated from the control room and the hot shutdown panel. These valves are


===.1 TI 2515/160 - Pressurizer Penetration Nozzles and Steam Space Piping Connections in===
required to shut in the event of a faulted steam generator or to prevent overfilling of a steam generator.


U.S. Pressurized Water Reactors
Description
:  The AFW system is an engineered safety feature system that is directly relied upon to prevent core damage and RCS overpressurization in the event of


====a. Inspection Scope====
transients, such as a loss of normal feedwater or secondary system pipe rupture. It also
The inspectors reviewed PG&E's actions regarding the inspection and repair associated with Alloy 82/182/600 material that may have been used in pressurizer penetration


nozzles, steam space piping connections, heads, and shells. Specifically, the inspectors
provides a means for plant cooldown following any plant transient.


reviewed PG&E's response to NRC Bulletin 2004-01, "Inspection of Alloy 82/182/600
Motor-operated Valves FW-1-LCV-107, FW-1-LCV-108, and FW-1-LCV-109 are discharge isolation valves associated with the turbine-driven AFW pump. On


Materials Used in the Fabrication of Pressurizer Penetrations and Steam Space Piping
March 15, 2003, Valve FW-2-LCV-109 failed to close during routine surveillance testing.


Connections at Pressurized Water Reactors."  PG&E documented in their response to
Operators failed to preserve the faulted condition by remotely opening the valve, manually stroking the valve, removing the actuator cover and inspecting the contacts, and burnishing the close torque contacts. Because the failure was not repeated during


the bulletin that the Unit 2 pressurizer utilized Alloy 82/182 material in the nozzle to safe
troubleshooting, PG&E staff determined that it was not a maintenance preventable


end welds for the surge line, the pressurizer safety lines, the power-operated relief valve
functional failure. However, PG&E staff identified in AR A0578562 that this was a critical
-35-lines, and the spray line. Stainless steel was used in all other pressurizer penetration welds. In PG&E's response to the bulletin, they committed to a bare metal visual exam


of all the welds that had Alloy 82/182 material.
component failure that should be prevented from recurring per Procedure ER1.ID1, "Equipment Reliability Process," Revision 1.


The inspectors reviewed PG&E's response to NRC Bulletin 2004-01 and observed their inspection activities for the Unit 2 pressurizer. The inspectors verified the qualifications
On August 20, 2004, Valve FW-1-LCV-107 failed to operate after corrective maintenance. PG&E staff identified in AR A0616766 that this failure was a maintenance


of personnel performing the bare metal exam and independently observed several of the
preventible functional failure and directed staff to implement actions to prevent


subject pressurizer penetration welds for evidence of boric acid deposits and the
recurrence. The corrective action identified was to revise Procedure MP E-53.10A, "Preventive Maintenance of Limitorque Operators," to include steps to burnish the torque


capability to perform the bare metal exam. The inspectors reviewed Procedure ISI VT 2-1, "Visual Examination During Section XI System Pressure Test,"
switch contacts, since the cause of the valve to stroke was determined to be corrosion.


Revision 0, during the inspection.
On November 3, 2005, operators were performing a functional test of Valve FW-1-LCV-107 per Procedure STP V-2U2D, "Exercising S/G No. 2 AFW Supply


The activities required in Temporary Instruction (TI) 2515/160 for Diablo Canyon Power Plant Unit 2 have been completed. Documents reviewed by the inspectors are listed in
Valves LCV-107 and LCV-108," Revision 4, after valve packing had been replaced.


the attachment. This TI is closed for Unit 2.
Motor-operated Valve FW-1-LCV-107 had been stroked open and closed successfully


====b. Findings====
from the control room. Operational control for the valve was then transferred to the Hot
No findings of significance were identified.
 
Shutdown Panel, the valve was opened and not able to be shut. A second attempt to


===.2 TI 2515/165 - Operational Readiness of Offsite Power and Impact on Plant Risk===
shut the valve was unsuccessful. Records of the subsequent visual inspection indicated


====a. Inspection Scope====
that the contact fingers were coated with debris, but not the contact surfaces.
The objective of TI 2515/165, "Operational Readiness of Offsite Power and Impact on Plant Risk," is to gather information to support the assessment of nuclear power plant


operational readiness of offsite power systems and impact on plant risk. During this
Maintenance records also indicated that the actuator cover was removed and the torque


inspection, the inspectors interviewed PG&E personnel, reviewed applicable procedures, and gathered information for further evaluation by the Office of Nuclear Reactor
switch contacts were burnished. The valve was declared operable after several


Regulation.
successful operations. PG&E staff identified this problem in AR A0650104 and again


====b. Findings====
directed that this problem be prevented from recurring.
No findings of significance were identified.


===.3 (Closed) Unresolved Item (URI) 05000275/05-05-03:===
On February 2, 2006, a similar failure occurred with Valve FW-1-LCV-108. This valve also had successful operations following maintenance with a subsequent failure.
Corrective Actions to Prevent Repetitive Failures of AFW Limitorque Valves


====a. Inspection Scope====
Troubleshooting by PG&E staff determined that the torque limit switch contacts had high
The inspectors performed additional inspection associated with this URI to determine any performance issues associated with design and maintenance practices regarding


Limitorque actuators. The inspectors also evaluated any extent of condition and/or
resistance. During troubleshooting efforts, the inspectors observed that the contact


generic impacts.
switch housing cover for the Limitorque Model SMB-000 actuators had been modified to


====b. Findings====
allow them to fit over the contact assembly more easily. The inspectors also observed
Introduction
-37-that, even with the modified cover, the installation and removal of the close-fitting cover rubbed against the wires. PG&E troubleshooting personnel determined that the screws
:  A Green, NRC-identified NCV was identified for the failure to correct a significant condition adverse to quality as required by 10 CFR Part 50, Appendix B,
-36-Criterion XVI, "Corrective Action."  Specifically, PG&E failed to preclude repetition of similar failures with Limitorque Model SMB-000 motor-operated valves in the AFW


system. The failure of these motor-operated valves affected the ability of the valves to
would loosen if the wires leading to the torque switch were moved.


be operated from the control room and the hot shutdown panel. These valves are
The inspectors verified that the installation of the cover and potential for screw loosening by wire movement could contribute to valves failing to actuate, which had not been


required to shut in the event of a faulted steam generator or to prevent overfilling of a steam generator.
previously evaluated by PG&E staff as a possible contributor to the failures of


Description
Valve FW-1-LCV-107. PG&E initiated a root cause evaluation into the failure of the
:  The AFW system is an engineered safety feature system that is directly relied upon to prevent core damage and RCS overpressurization in the event of


transients, such as a loss of normal feedwater or secondary system pipe rupture. It also
Model SMB-000 actuators (Nonconformance Report NCR N0002205) and identified


provides a means for plant cooldown following any plant transient.
organizational deficiencies in the failure analysis of critical components as the root


Motor-operated Valves FW-1-LCV-107, FW-1-LCV-108, and FW-1-LCV-109 are discharge isolation valves associated with the turbine-driven AFW pump. On
cause. The root cause determined that PG&E staff failed to account for maintenance


March 15, 2003, Valve FW-2-LCV-109 failed to close during routine surveillance testing.
practices, latent design issues, or environmental effects other than corrosion to prevent


Operators failed to preserve the faulted condition by remotely opening the valve, manually stroking the valve, removing the actuator cover and inspecting the contacts, and burnishing the close torque contacts. Because the failure was not repeated during
repeat failures of Model SMB-000 actuators.


troubleshooting, PG&E staff determined that it was not a maintenance preventable
The inspectors determined that PG&E staff failed to promptly identify and correct a significant condition adverse to quality. Specifically, the inspectors determined that


functional failure. However, PG&E staff identified in AR A0578562 that this was a critical
PG&E failed to adequately troubleshoot the failures of Valve FW-1-LCV-107. During the


component failure that should be prevented from recurring per Procedure ER1.ID1, "Equipment Reliability Process," Revision 1.
inspection, data such as:
: (1) the failure of the valves to stroke after one or more


On August 20, 2004, Valve FW-1-LCV-107 failed to operate after corrective maintenance. PG&E staff identified in AR A0616766 that this failure was a maintenance
successful strokes,
: (2) the conductance capability of the silver torque switch contacts


preventible functional failure and directed staff to implement actions to prevent
with corrosion,
: (3) the orientation of the torque switch contacts, and
: (4) an already


recurrence. The corrective action identified was to revise Procedure MP E-53.10A, "Preventive Maintenance of Limitorque Operators," to include steps to burnish the torque
present step in the maintenance procedure to clean the torque switch contacts lead the


switch contacts, since the cause of the valve to stroke was determined to be corrosion.
inspectors to question the troubleshooting conclusion of debris or corrosion on the


On November 3, 2005, operators were performing a functional test of Valve FW-1-LCV-107 per Procedure STP V-2U2D, "Exercising S/G No. 2 AFW Supply
torque switch contacts. Furthermore, the troubleshooting results from


Valves LCV-107 and LCV-108," Revision 4, after valve packing had been replaced.
Valve FW-1-LCV-108 reduced the likelihood of debris or corrosion as a possible failure


Motor-operated Valve FW-1-LCV-107 had been stroked open and closed successfully
mechanism. The inspectors determined that, with the history of similar failures of these


from the control room. Operational control for the valve was then transferred to the Hot
type of valve actuators, along with the si gnificance of the system, PG&E should have initiated a root cause evaluation earlier with the Valve FW-1-LCV-107 failures to prevent


Shutdown Panel, the valve was opened and not able to be shut. A second attempt to
recurrence of the problem.


shut the valve was unsuccessful. Records of the subsequent visual inspection indicated
=====Analysis:=====
The performance deficiency associated with this finding was the failure to promptly identify and correct a significant condition adverse to quality associated with


that the contact fingers were coated with debris, but not the contact surfaces.
the AFW motor-operated discharge valves. The finding is greater than minor because it


Maintenance records also indicated that the actuator cover was removed and the torque
is associated with the Mitigating Systems Cornerstone attribute of equipment


switch contacts were burnished. The valve was declared operable after several
performance and affects the associated cornerstone objective to ensure the availability, reliability, and capability of systems that respond to initiating events to prevent


successful operations. PG&E staff identified this problem in AR A0650104 and again
undesirable consequences. Using the IMC 0609, "Significance Determination Process,"


directed that this problem be prevented from recurring.
Phase 1 Worksheet, the finding is determined to be of very low safety significance


On February 2, 2006, a similar failure occurred with Valve FW-1-LCV-108. This valve also had successful operations following maintenance with a subsequent failure.
because it did not represent an actual loss of safety function, represent an actual loss of


Troubleshooting by PG&E staff determined that the torque limit switch contacts had high
safety function for a single train for greater than the TS allowed outage time, or screen


resistance. During troubleshooting efforts, the inspectors observed that the contact
as potentially risk significant due to seismic, fire, flooding, or severe weather initiating


switch housing cover for the Limitorque Model SMB-000 actuators had been modified to
events. The finding had a crosscutting aspect in the area of problem identification and


allow them to fit over the contact assembly more easily. The inspectors also observed
resolution since PG&E staff failed to adequately trend, assess, and troubleshoot
-37-that, even with the modified cover, the installation and removal of the close-fitting cover rubbed against the wires. PG&E troubleshooting personnel determined that the screws


would loosen if the wires leading to the torque switch were moved.
previous Limitorque SMB-000 actuator failures.


The inspectors verified that the installation of the cover and potential for screw loosening by wire movement could contribute to valves failing to actuate, which had not been
=====Enforcement:=====
10 CFR Part 50, Appendix B, Criterion XVI, states, in part, that measures shall be established to assure that conditions adverse to quality, such as failures, malfunctions, deficiencies, deviations, defective material and equipment, and


previously evaluated by PG&E staff as a possible contributor to the failures of
nonconformances, are promptly identified and corrected. In the case of significant


Valve FW-1-LCV-107. PG&E initiated a root cause evaluation into the failure of the
conditions adverse to quality, the measures shall assure that the cause of the condition
-38-is determined and corrective action taken to preclude repetition. Contrary to this, from 2003 to 2006, PG&E staff failed to identify and implement adequate corrective actions to


Model SMB-000 actuators (Nonconformance Report NCR N0002205) and identified
prevent recurrence of turbine-driven AFW Limitorque SMB-000 actuator failures. Since


organizational deficiencies in the failure analysis of critical components as the root
failure to identify and prevent recurrence of a significant condition adverse to quality was


cause. The root cause determined that PG&E staff failed to account for maintenance
determined to be of very low safety significance and has been entered into the CAP as


practices, latent design issues, or environmental effects other than corrosion to prevent
Nonconformance Report N0002205, this violation is being treated as a NCV, consistent


repeat failures of Model SMB-000 actuators.
with Section VI.A of the NRC Enforcement Policy:  NCV 50-275/06-03-05, Failure to


The inspectors determined that PG&E staff failed to promptly identify and correct a significant condition adverse to quality. Specifically, the inspectors determined that
Prevent Recurrence of Limitorque Model SMB-000 Failures.40A6Management Meetings


PG&E failed to adequately troubleshoot the failures of Valve FW-1-LCV-107. During the
===Exit Meeting Summary===


inspection, data such as:
On April 6, 2006, the inspectors discussed the inspection results of licensed operator requalification with Mr. David Burns, Operations Training Supervisor. PG&E
: (1) the failure of the valves to stroke after one or more


successful strokes,
acknowledged the findings presented. The inspectors asked PG&E if any materials
: (2) the conductance capability of the silver torque switch contacts


with corrosion,
examined during the inspection should be considered proprietary. No proprietary
: (3) the orientation of the torque switch contacts, and
: (4) an already


present step in the maintenance procedure to clean the torque switch contacts lead the
information was identified.


inspectors to question the troubleshooting conclusion of debris or corrosion on the
On April 10, 2006, the inspectors conducted a telephonic exit meeting to present the inspection results on Emergency Action Level and Emergency Plan Changes to


torque switch contacts. Furthermore, the troubleshooting results from
Mr. R. Waltos, Supervisor, Emergency Planning, who acknowledged the findings. The


Valve FW-1-LCV-108 reduced the likelihood of debris or corrosion as a possible failure
inspectors confirmed that proprietary info rmation was not provided or examined during the inspection.


mechanism. The inspectors determined that, with the history of similar failures of these
The inspector presented the results of the inservice inspection effort to Mr. J. Becker, Vice President Diablo Canyon Operations and Station Director, and other members of


type of valve actuators, along with the si gnificance of the system, PG&E should have initiated a root cause evaluation earlier with the Valve FW-1-LCV-107 failures to prevent
PG&E management on May 3, 2006. PG&E management acknowledged the inspection


recurrence of the problem.
findings. During the inspection, the inspector asked if any materials examined should be


=====Analysis:=====
considered proprietary. Several documents were identified as proprietary information by
The performance deficiency associated with this finding was the failure to promptly identify and correct a significant condition adverse to quality associated with


the AFW motor-operated discharge valves. The finding is greater than minor because it
PG&E. The inspector informed PG&E that copies of those documents would be


is associated with the Mitigating Systems Cornerstone attribute of equipment
destroyed after their review.


performance and affects the associated cornerstone objective to ensure the availability, reliability, and capability of systems that respond to initiating events to prevent
On May 4, 2006, the inspectors presented the occupational radiation safety inspection results to Mr. J. Becker, Vice President Diablo Canyon Operations and Station Director, and other members of the staff who acknowledged the findings. The inspectors


undesirable consequences. Using the IMC 0609, "Significance Determination Process,"
confirmed that proprietary information was not provided or examined during the inspection.


Phase 1 Worksheet, the finding is determined to be of very low safety significance
The resident inspection results were presented on July 12, 2006, to Mr. J. Becker, Vice President Diablo Canyon Operations and Station Director, and other members of PG&E


because it did not represent an actual loss of safety function, represent an actual loss of
management. PG&E acknowledged the findings presented. The inspectors asked


safety function for a single train for greater than the TS allowed outage time, or screen
PG&E whether any materials examined during the inspection should be considered


as potentially risk significant due to seismic, fire, flooding, or severe weather initiating
proprietary. No proprietary information was reviewed by the inspectors.


events. The finding had a crosscutting aspect in the area of problem identification and
ATTACHMENT: 


resolution since PG&E staff failed to adequately trend, assess, and troubleshoot
=SUPPLEMENTAL INFORMATION=


previous Limitorque SMB-000 actuator failures.
==KEY POINTS OF CONTACT==


=====Enforcement:=====
PG&E personnel
10 CFR Part 50, Appendix B, Criterion XVI, states, in part, that measures shall be established to assure that conditions adverse to quality, such as failures, malfunctions, deficiencies, deviations, defective material and equipment, and
 
nonconformances, are promptly identified and corrected. In the case of significant
 
conditions adverse to quality, the measures shall assure that the cause of the condition
-38-is determined and corrective action taken to preclude repetition. Contrary to this, from 2003 to 2006, PG&E staff failed to identify and implement adequate corrective actions to
 
prevent recurrence of turbine-driven AFW Limitorque SMB-000 actuator failures. Since
 
failure to identify and prevent recurrence of a significant condition adverse to quality was
 
determined to be of very low safety significance and has been entered into the CAP as
 
Nonconformance Report N0002205, this violation is being treated as a NCV, consistent
 
with Section VI.A of the NRC Enforcement Policy:  NCV 50-275/06-03-05, Failure to
 
Prevent Recurrence of Limitorque Model SMB-000 Failures.40A6Management Meetings
 
===Exit Meeting Summary===
 
On April 6, 2006, the inspectors discussed the inspection results of licensed operator requalification with Mr. David Burns, Operations Training Supervisor. PG&E
 
acknowledged the findings presented. The inspectors asked PG&E if any materials
 
examined during the inspection should be considered proprietary. No proprietary
 
information was identified.
 
On April 10, 2006, the inspectors conducted a telephonic exit meeting to present the inspection results on Emergency Action Level and Emergency Plan Changes to
 
Mr. R. Waltos, Supervisor, Emergency Planning, who acknowledged the findings. The
 
inspectors confirmed that proprietary info rmation was not provided or examined during the inspection.
 
The inspector presented the results of the inservice inspection effort to Mr. J. Becker, Vice President Diablo Canyon Operations and Station Director, and other members of
 
PG&E management on May 3, 2006. PG&E  management acknowledged the inspection
 
findings. During the inspection, the inspector asked if any materials examined should be
 
considered proprietary. Several documents were identified as proprietary information by
 
PG&E. The inspector informed PG&E that copies of those documents would be
 
destroyed after their review.
 
On May 4, 2006, the inspectors presented the occupational radiation safety inspection results to Mr. J. Becker, Vice President Diablo Canyon Operations and Station Director, and other members of the staff who acknowledged the findings. The inspectors
 
confirmed that proprietary information was not provided or examined during the inspection.
 
The resident inspection results were presented on July 12, 2006, to Mr. J. Becker, Vice President Diablo Canyon Operations and Station Director, and other members of PG&E
 
management. PG&E acknowledged the findings presented. The inspectors asked
 
PG&E whether any materials examined during the inspection should be considered
 
proprietary. No proprietary information was reviewed by the inspectors.
 
ATTACHMENT: 
 
=SUPPLEMENTAL INFORMATION=
 
==KEY POINTS OF CONTACT==
 
PG&E personnel
: [[contact::J. Becker]], Vice President - Diablo Canyon Operations and Station Director
: [[contact::J. Becker]], Vice President - Diablo Canyon Operations and Station Director
: [[contact::S. David]], Manager, Operations
: [[contact::S. David]], Manager, Operations
Line 2,087: Line 1,999:


===Closed===
===Closed===
: 05000275/2005-05-03URICorrective Actions to Prevent Repetitive Failures of
05000275/2005-05-03URICorrective Actions to Prevent Repetitive Failures of
: Auxiliary Feedwater Limitorque Valves  
Auxiliary Feedwater Limitorque Valves  
: A-250-275/1-2005-001-00LERSteam Generator Tube Plugging Because of Stress
 
: Corrosion Cracking (Section 4OA3.1)
A-250-275/1-2005-001-00LERSteam Generator Tube Plugging Because of Stress
Corrosion Cracking (Section 4OA3.1)


==LIST OF DOCUMENTS REVIEWED==
==LIST OF DOCUMENTS REVIEWED==
==Section 1R04: ==
: Equipment Alignment (71111.04)
: Action RequestsA0606585A0634661A0661369
===Procedures===
: Number Title RevisionSTP M-12AVital Station Battery Modified Performance Test14OP J-9:IPlacing the 125/250V DC System In Service4
: OP H-10:IAuxiliary Building Switchgear Ventilation System - Make Available and System Operation
: 27APEP
: EN-1Plant Accident Mitigation Diagnostic Aids and Guidelines15EOP E-1.2Post LOCA Cooldown and Depressurization16
: OP
: AP-26Loss of Offsite Power8
===Other Documents===
: Calculation 786, Appendix A, "EDG Fuel Oil Storage," Revision 14
: IEEE 450-1995, "IEEE Recommended Practice for Maintenance, Testing, and Replacement of Large Lead Storage Batteries for Generating Stations and Substations."
==Section 1R06: ==
: Flood Protection (71111.06)
: Action RequestsA0448720A0457845A0497879A0525555A0529058A0571204A0598359A0620636A0630476A0630513A0635450A0651267
: A0663041 Work Orders
: R0271922
==Section 1R08: Inservice Inspection Activities (71111.08)==
: PG&E ProceduresNumber Title RevisionMP-56.10Piping Fabrication, Installation, Repair or System Alteration16MA3.DC1Weld Planning and Inspection6
: SWS-1Welding in the Presence of Moisture2
: GWS-ASMEASME General Welding Standard8
: WI-1Visual Inspection of Welds7
: ISI MONITORInspection of Nondestructive Examination Activities1
: ISI ADD SUCCESSAdditional and Successive Inspections1STP M-SGTISteam Generator Tube Inspections12TS1.ID3Steam Generator Management Program0
: ER1.ID2Boric Acid Corrosion Control Program1
: AD4.ID2Plant Leakage Evaluation6
: STP R-8CContainment Walkdown for Evidence of Boric Acid Leakage8A
: WESDYNE Procedures Number Title RevisionWDI-ET-002Intraspect Eddy Current Inspection of Vessel Head Penetrations
: J-Weld and Tube OD
: 7WDI-ET-003Intraspect Eddy Current Imaging Procedure for Inspection of Reactor Vessel Head Penetrations
: 9WDI-ET-004Instraspect Eddy Current Analysis Guidelines10PDI-ISI-254Remote In-service Inspection of Reactor Vessel Shell Welds7
: PDI-ISI-254-NZRemote In-service Examination of Reactor Vessel Nozzle to Shell Welds
: 0PDI-ISI-254-SERemote In-service Examination of Reactor Vessel Nozzle to Safe End, Nozzle to Pipe, and Safe End to Pipe Welds Action
: RequestsA0665682A0665588A0665547A0665543A0665166
: Work OrdersC0196956C0194616C0198594
: Visual Examination Steam Generator 1 Feedwater Supply Hanger 2037-7V
: Auxiliary Feedwater Pump 2-1 Discharge Header Hanger 414-505R
: Auxiliary Feedwater Pump 2-1 Discharge Header Hanger 414-386R
: Auxiliary Feedwater Supply Hanger 42-42R
: Radiographic Examination
: CVCS-2-8388C,
: FW-2
: Magnetic Particle Examination
: K16-555-16
: K16-557-16
: Liquid Penetrant Examination
: S6-959-2 SPL WIB-503
: S6-959-2 SPL
: WIB-1009
===Calculations===
: Structural Integrity Associates, Inc. Calculation Package
: PGE-120Q-301,"ASME Code SectionXI Flaw Evaluation of Indication in RHR Piping Weld
: RB-119-11," Revision 0
==Section 1R12: ==
: Maintenance Effectiveness (71111.12)
: Action RequestsA0556053A0649534A0650238A0651876A0603817A0650052A0650418A0658073
===Documents===
: Number Title RevisionNUMARC 93-01Industry Guideline for Monitoring the Effectiveness of Maintenance at Nuclear Power Plants
: 2Reg. Guide 1.160Monitoring the Effectiveness of Maintenance at Nuclear Power Plants
===Procedures===
: Number Title RevisionSTP V-600General Containment Isolation Valve Leak Tests20STP V-623Penetration 22 and 23 Containment Isolation Valve Leak Test 11
==Section 1R13: ==
: Maintenance Risk Assessments and Emergent Work Control (71111.13)
: Action RequestsA0500194A0636681A0657460A0660735A0660739A0660743A0660745A0660759A0660769A0662536A0669224
===Procedures===
: Number Title RevisionAD7.DC6On-line Maintenance Risk Management9MA1.DC11Risk Assessment7
: OP J-6B:IXDiesel Generator Extended On-Line Maintenance0
: STP M-75G4kV Vital Bus G Undervoltage Relay Calibration28
: Work OrdersC0187543R0253468R0257749C0203401
==Section 1R14: ==
: Personnel Performance Related to Nonroutine Plant Evolutions and Events (71111.14)
: Action RequestsA0669566A0672188
: DocumentsNumberTitleRevision Operations Policy C-7Earthquakes2MP E-50.45Qualitrol Type "900" Rapid Response Pressure Relay Maintenance
===Work Orders===
: C0204748
: A-7
==Section 1R15: ==
: Operability Evaluations(71111.15)
: Action RequestsA0663750A0663823A0657428A0668922A0668929A0669468A0669453A0669270A0640357A0666128A0666211A0666438
: A0666532A0666701A0666717A0666761A0667468A0669872
===Drawings===
: Number Sheet Title Revision1067092Safety Injection System44437984Unit 1 Accumulator Injection Loop No. 3 - Design Review Isometric 11445889Injection Line for Loop 3 Accumulator 2-3 - Design Review Isometric 5437547Single Line Meter and Relay Diagram 120V Instrument AC
: System 38 Procedures Number Title RevisionAR
: PK 19-18Vital UPS Trouble3AR
: PK 19-19Vital UPS Failure1A
: MP E-65.1AMaintenance and Overhaul of Solidstate Controls 20 kVA
: UPS 25MP I-2.29-1Capacitor Capacitance and Leakage Testing5OP-J-10:IVInstrument AC System - Transfer of Vital Panel Power Supply 22PEP M-98ASetting final Feedwater Flow Nozzles by "AMAG" Crossflow15STP M-78CTransient Event Evaluation2
: TP
: TB-0616Emergency Core Cooling System Cold Leg Check Valve Test of
: SI-2-8956C0XPR
: Work OrdersR0116149C0204222
===Other Documents===
: Operations Shift Log, Unit 1, Sunday Dayshift, November 27, 2005
: Operations Shift Log, Unit 2, Sunday Dayshift, May 21, 2006
: PGE-120Q-301, "Flaw Evaluation of Diablo Canyon Unit 2 Residual Heat Removal System Weld," dated April 4, 2006
: NUREG-0927, "Evaluation of Water Hammer Occurrence in Nuclear Power Plants," Revision 1
: Engineering Drawing Transmittals:
: 31345, 31346, 31347, and 31348, Revision 0
: Technical Manual: DC6013738-1-2, "Operation-Maintenance Instructions for 1 20kVA UPS
with Regulating Rectifier," Revision 1
: Email from John Miemi to Rudy Ortega, dated June 16, 2005, RE: 2-pole relays
==Section 1R17: Permanent Plant Modifications (71111.17)==
===Action Requests===
: A0652663 DocumentsEngineering Drawing Transmittal 30931, "Modify the 3/16" X 3/16" Mesh Screen of the RHR
: Inner Screen," Revision 0, dated January 3, 2006
: DCM S-9A, Revision 4, Pages 32-35, "Containment Recirculation Pump Function"
===Vendor Document===
: 663216, "Evaluation of the Potential Hydraulic Performance of the Containment Recirculation Sumps," Revision 3, dated February 26, 2002
: Regulatory Guide 1.82, "Water Sources for Long-term Recirculation Cooling Following a Loss-
of-coolant Accident," Revision 3, November, 2003
===Calculations===
: M-580, "Determination of Post LOCA Flood Levels Inside Containment Buildings for Units 1 and
: 2," Revision 4, Dated September 2, 1997
: M-227, "Post-LOCA Minimum Containment Sump Level," Revision 4, Dated February 28, 2006 
===Drawings===
: Number Title Revision4004934Sections and Details Recirculation Sump Screens Area "C" Containment Structure
: 34004935Recirculation Sump Screens Area "G" Containment Structure14004936Plans, Sections and Details Recirculation Sump Screens Area "G" Containment Structure
: 3438208Recirculation Sump Screens Area "G" Containment Structure4498837Plans, Sections and Details Recirculation Sump Screens Area "G" Containment Structure
: 5498838Plans, Sections and Details Recirculation Sump Screens Area "G" Containment Structure
: 56001027Recirculation Sump Screen Mod's26002061Elevation 91' -0" Recirculation Sump Screens Containment Structure 2
: 6016131, Sheet 1RHR Recirculation Sump Screen Addition Demolition Plan0
: 6016131, Sheet 2 RHR Recirculation Sump Screen Addition Plan, Sections &
: General Notes
: 6016131, Sheet 5RHR Recirculation Sump Addition Demolition Plan1
: 6016131, Sheet 6 RHR Recirculation Sump Screen Addition Plan, Sections &
: General Notes
: 6016131, Sheet 8RHR Recirculation Sump Screen Addition Sections & Details1
==Section 1R19: ==
: Postmaintenance Testing Action RequestsA0402074A0664845A0666578A0666599A0670676A0616738A0665900A0666579A0667681 
===Procedures===
: Number Title RevisionMP E-57.14API and HIPOT Testing19MP E-57.15Maintenance and Calibration of Ammeters, Voltmeters, Frequency Meters and Tachometers
: 9MP E-65.1AMaintenance and Overhaul of Solidstate Controls 20 KVA
: UPS 29OP B-8DS1Core Offloading35PEP I-17-FIT-484ASW Magnetic Flowmeters
: FE-484 and
: FE-485 Flow Rate Comparision Test
: 1PMT 63.5152HH13 Auxiliary Transformer 22 Hinge Wire Replacement0STP I-4AAnalog Channel Operational Test Nuclear Source Range29A
: STP I-4BCalibration of Source Range Channels7
: STP I-4B1Removal of a Source Range Channel from Service17A
: STP I-4B2Calibration Procedure for Source Range Channel23A
: STP I-4B4Determ of Source Range Detector Characteristic Curves for Westinghouse Low Noise Preamplifiers
: 16STP M-27BFuel Transfer System Interlock Verification and Functional Testing 8STP P-ASW-APerformance Test of Auxiliary Saltwater Pumps22STP P-CCP-A21Comprehensive Pump Test for Centrifugal Charging Pump 2-1 1 Other Documents Calculation
: STA-228, "Safety Injection System - 2R13 CCP 2-1 Evaluation," Revision 0
: Field Correction Transmittal Form 31333, "As built drawing
: 441595 for Unit 2 4kV cubicle 52-
: HH-13," Revision 0
: Drawing
: 441595, "Electrical Wiring Diagram 4 KV Switchgear Bus Section "H" Cell 13," Revision 12
: Work OrdersC0204016R0221536R0254405R0266353C0204027R0244739R0264682R0269399
==Section 2OS1: Access Controls to Radiologically Significant Areas (71121.01)==
: Action RequestsA0658441A0659687A0660724A0661344A0662965A0663482A0663517A0664429A0664703A0665039A0665254A0666110
: A0666292A0666296
===Procedures===
: Number Title RevisionOM7.ID1Problem Identification and Resolution-Action Requests22RCP D-211Control of Work in Radiologically Significant Areas2
: RCP D-220Control of Access to High, Locked High, and Very High Radiation Areas
: 31RCP D-222Radiation Protection Lock and Key Control4RCP D-230Radiological Control for Containment Entry16
: RCP D-240Radiological Posting16
: RCP D-420Sampling and Measurement of Airborne Radioactivity18A
: RCP D-430Plant Airborne Radioactivity Surveillance16
: RCP D-440Criteria for Use and Operation of HEPA Equipped Ventilation Units 1RCP D-500Routine and Job Coverage Surveys21
: Radiation Work Permits06-0010Routine Operations Activities06-20192R13 Fuel Handling at the Spent Fuel Pool
: 06-20222R13 Movement of Reactor Head and Upper Internals
: 06-20232R13 Fuel Movement and Underwater Work in Containment
: 06-20262R13 Lower Cavity and Transfer Canal Work
: 06-20402R13 Primary Steam Generator Setup and Teardown
: 206-20602R13 Pressurizer Relief Maintenance06-20642R13 Non-Containment Valves & Breaches Less Than 100 mrem Per Entry
: 06-20712R13 Reactor Upflow-UHTR Modifications
: 06-20732R13 Under Reactor Head Volumetric Inspection
: 06-20842R13 Reactor Vessel Flange and Stud Hole Inspection
==Section 2OS2: ==
: ALARA Planning and Controls (71121.02)
: Action RequestsA0666290 A0663205 A0663913 A0663953 A0664432 A0664430 A0659218
===Procedures===
: Number Title Revisio nRCP D-200Writing Radiation Work Permits34RP1.ID1Requirements for the ALARA Program2C
: RP1.ID2Use and Control of Temporary Radiation Shielding5B
: RP1.ID3Respiratory Protection Program6
: RP1.DC4Radiological Hot Spot Identification and Control Program1A
==Section 4OA1: Performance Indicator Verification (71151)==
===Action Requests===
: A0658441 Procedures Number Title Revisio nAWP O-003NRC Performance Indicators: Occupation Exposure Control Effectiveness
==4XI1 .DC1Collection and Submittal of==
: NRC Performance Indicators6
==Section 4OA2: ==
: Identification and Resolution of Problems (71152)
: Action RequestsA0024144A0169950A0239973A0302261A0593433A0647639A0039958A0174572A0246479A0433356A0617930A0647640
: A0086712A0196328A0259649A0434508A0617931A0665174
: A0146446A0198060A0270757A0446881A0623598A0667224
: A0150563A0235288A0279415A0514587A0626219A0671308
: A0152429A0238661A0284544A0566264A0635891A0238665
: A0161566A0239954A0299519A0579166A0638342A0568834
===Documents===
: Design Control Manual S-23B, Main Auxiliary Building Heating and Ventilating System, Revision 20
: Design Control Manual T-20, Environmental Qualification, Revision 8
: Equipment Control Guidelines, Section 23.1, Area Temperature Monitoring, Revision 2
: Drawing DC663213-22, CCW Motor Outline Drawing, Revision 5
===Procedure===
: AR PK01-09, CCW Pumps, Revision 6
==Section 4OA3: Event Followup==
===Action Requests===
: A0669689 Procedures
: OP C-3:II, "Main Unit Turbine - Startup," Revision 31
: OP L-3, "Secondary Plant Startup," Revision 32


==Section 4OA5: ==
: Other ProceduresISI VT 2-1, "Visual Examination During Section XI System Pressure Test," Revision 0
==LIST OF ACRONYMS==
ADAMSagency document and management systemAFWauxiliary feedwater
ALARAas low as is reasonably achievable
ARaction request
ASMEAmerican Society of Mechanical Engineers
: [[CAP]] [[corrective action program]]
: [[CFR]] [[Code of Federal Regulations]]
EPRIElectric Power Research Institute
FSARFinal Safety Analysis Report
IMCInspection Manual Chapter
NCVnoncited violation
NDEnondestructive examination
NEINuclear Energy Institute
NRCNuclear Regulatory Commission
PARSPublicly Available Records System
PG&EPacific Gas and Electric Company
PIperformance indicator
RCSreactor coolant system
RVRLISreactor vessel refueling level indication system
SSCstructure, system, and component
TItemporary instruction
TSTechnical Specifications
URIunresolved item
: [[VUHP]] [[vessel upper head penetration]]
}}
}}

Revision as of 13:14, 13 July 2019

IR 05000275-06-003, 05000323-06-003; 4/1/06 - 6/30/06; Diablo Canyon Power Plant Units 1 and 2; Inservice Inspection Activities, Operability Evaluations, Refueling and Outage Activities, and Access Control to Radiologically Significant Area
ML062270051
Person / Time
Site: Diablo Canyon  Pacific Gas & Electric icon.png
Issue date: 08/14/2006
From: William Jones
NRC/RGN-IV/DRP/RPB-B
To: Keenan J
Pacific Gas & Electric Co
References
IR-06-003
Download: ML062270051 (59)


Text

August 14, 2006 John Senior Vice President - Generation

and Chief Nuclear Officer

Pacific Gas and Electric Company

P.O. Box 770000

Mail Code B32

San Francisco, CA 94177-0001SUBJECT:DIABLO CANYON POWER PLANT - NRC INTEGRATED INSPECTION REPORT 05000275/2006003 AND 05000323/2006003

Dear Mr. Keenan:

On June 30, 2006, the U.S. Nuclear Regulatory Commission completed an inspection at your Diablo Canyon Power Plant, Units 1 and 2, facility. The enclosed integrated report documents

the inspection findings that were discussed on July 12, 2006, with Mr. James Becker and

members of your staff.

This inspection examined activities conducted under your licenses as they relate to safety and compliance with the Commission's rules and regulations and with the conditions of your

licenses. The inspectors reviewed selected procedures and records, observed activities, and

interviewed personnel.

There were four NRC-identified findings and one self-revealing finding of very low safety significance (Green) identified in this report. These findings involved violations of NRC

requirements. However, because of their very low risk significance and because they are

entered into your corrective action program, the NRC is treating these five findings as noncited

violations (NCVs) consistent with Section VI.A of the NRC Enforcement Policy. If you contest any NCV in this report, you should provide a response within 30 days of the date of this

inspection report, with the basis for your denial, to the U.S. Nuclear Regulatory Commission, ATTN: Document Control Desk, Washington, DC 20555-0001; with copies to the Regional

Administrator, U.S. Nuclear Regulatory Commission, Region IV, 611 Ryan Plaza Drive, Suite

400, Arlington, Texas 76011-4005; the Director, Office of Enforcement, U.S. Nuclear Regulatory

Commission, Washington, DC 20555-0001; and the NRC Resident Inspector at the Diablo

Canyon Power Plant.

Pacific Gas and Electric Company- 2 -

In accordance with 10 CFR 2.390 of the NRC's "Rules of Practice," a copy of this letter and its enclosure will be available electronically for public inspection in the NRC Public Document

Room or from the Publicly Available Records (PARS) component of NRC's document system (ADAMS). ADAMS is accessible from the NRC Web site at http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room).

Sincerely,

/RA/William B. Jones, Chief Project Branch B

Division of Reactor Projects Dockets: 50-275 50-323

Licenses: DPR-80

DPR-82

Enclosure:

Inspection Report 05000275/2006003

and 05000323/2006003

w/attachment: Supplemental Information

REGION IVDockets:50-275, 50-323 Licenses:DPR-80, DPR-82 Report:05000275/2006003 05000323/2006003Licensee:Pacific Gas and Electric Company (PG&E)

Facility:Diablo Canyon Power Plant, Units 1 and 2 Location:7 1/2 miles NW of Avila Beach Avila Beach, CaliforniaDates:April 1 through June 30, 2006 Inspectors:T. Jackson, Senior Resident Inspector T. McConnell, Resident Inspector

S. Graves, Reactor Inspector

P. Gage, Senior Operations Engineer

R. Lantz, Senior Emergency Preparedness Inspector

J. Tapia, Senior Reactor Inspector

B. Tharakan, Health PhysicistApproved By:W. B. Jones, Chief, Project Branch B Division of Reactor Projects Enclosure-2-

SUMMARY OF FINDINGS

IR 05000275/2006-003, 05000323/2006-003; 4/1/06 - 6/30/06; Diablo Canyon Power Plant

Units 1 and 2; Inservice Inspection Activities, Operability Evaluations, Refueling and Outage

Activities, and Access Control to Radiologically Significant Areas.

This report covered a 13-week period of inspection by resident inspectors and announced inspections in radiation protection, emergency preparedness, operator requalification, and in-

service inspections. One self-revealing and four NRC-identified, Green, noncited violations were identified. The significance of most findings is indicated by their color (Green, White,

Yellow, or Red) using Inspection Manual Chapter 0609, "Significance Determination Process."

Findings for which the Significance Determination Process does not apply may be Green or be assigned a severity level after NRC management review. The NRC's program for overseeing the safe operation of commercial nuclear power reactors is described in NUREG-1649, "Reactor

Oversight Process," Revision 3, dated July 2000.A.

NRC-Identified and Self-Revealing Findings

Cornerstone: Mitigating Systems

Green.

A self-revealing, noncited violation of 10 CFR Part 50, Appendix B,Criterion XVI, was determined for the failure of operations personnel to promptly identify a condition adverse to quality. Specifically, on November 27, 2005, operators failed to document, in the corrective action program, an unexpected level drop in Accumulator 1-3. Failure to enter the occurrence into the corrective action program precluded actions that would have addressed similar conditions that resulted in a subsequent event involving an unexpected level drop and water hammer associated with Accumulator 2-3, which occurred on May 21, 2006.

This issue was entered into Pacific Gas and Electric Company's corrective action program as Action Request A0669468.

The finding is greater than minor because it is associated with the Mitigating Systems Cornerstone attribute of configuration control and affects the associated cornerstone objective to ensure the availability, reliability, and capability of systems that respond to initiating events to prevent undesirable consequences.

Using the Inspection Manual Chapter 0609, "Significance Determination

Process," Phase 1 Worksheet, the finding is determined to be of very low safety significance because the finding did not represent a loss of a safety function, an actual loss of a safety-related train for greater than its Technical Specification allowed outage time, or screen as potentially risk-significant due to seismic, fire, flooding, or severe weather initiating events. The finding had a crosscutting aspect in the area of problem identification and resolution because operations personnel failed to promptly identify, in the corrective action program, the unexpected level drop in Accumulator 1-3 (Section 1R15).*Green. An NRC-identified, noncited violation of Technical Specification 5.4.1.a for an inadequate procedure, Procedure OP A-2:II, "Reactor Vessel - Draining the RCS to the Vessel Flange - With Fuel in Vessel," Revision 33A. Specifically, on April 20, 2006, while operators depressurized the reactor coolant system, with Enclosure-4-water level 2 feet below the reactor vessel flange, the two required level instruments, wide-range reactor vessel refueling level indication system and

LI-400, read 15 inches higher than actual reactor vessel water level. The inspectors determined that the procedure was not adequate because prior operating experience had not been incorporated into the procedure that demonstrated the level instruments would read nonconservatively during the reactor coolant system depressurization. Also, Procedure OP A-2:II did not have criteria that alerted operators to abnormal level instrument deviations that may be caused by phenomenon outside of the level deviations expected by the reactor coolant system depressurization. Pacific Gas and Electric Company has planned to evaluate potential changes to Procedure OP A-2:II and reactor coolant system water level instrumentation when used during reactor coolant system depressurization. This issue was entered into Pacific Gas and Electric

Company's corrective action program as Action Requests A0664484, A0672419, and A0672422.

The finding is greater than minor because it is associated with the Mitigating Systems Cornerstone attribute of procedure quality and affects the associated cornerstone objective to ensure the availability, reliability, and capability of systems that respond to initiating events to prevent undesirable consequences.

Using Inspection Manual Chapter 0609, Appendix G, Attachment 1, Checklist 3, the finding is determined to be of very low safety significance since an optional set of instrumentation provided accurate reactor coolant system level indication and there was no loss of reactor coolant system inventory control. The finding had a crosscutting aspect in the area of human performance for resources because Pacific Gas and Electric Company failed to ensure the adequacy of procedures used for reactor vessel level monitoring to ensure nuclear safety (Section 1R20).*Green. An NRC-identified noncited violation of 10 CFR Part 50, Criterion XVI,"Corrective Actions," was determined for the failure to prevent recurrence of a similar failures, that occurred between 2003 and 2006, of Limitorque SMB-000 actuators in the auxiliary feedwater sy stem. Pacific Gas and Electric Company staff failed to adequately troubleshoot and provide for timely corrective actions regarding auxiliary feedwater control valves that failed due to high actuator torque switch resistance. This finding was entered into Pacific Gas and Electric

Company's corrective action program as Nonconformance Report N0002205.

The finding is greater than minor because it is associated with the Mitigating Systems Cornerstone attribute of equipment performance and affects the associated cornerstone objective to ensure the availability, reliability, and capability of systems that respond to initiating events to prevent undesirable consequences. Using the Inspection Manual Chapter 0609, "Significance

Determination Process," Phase 1 Worksheet, the finding is determined to be of very low safety significance because it did not represent an actual loss of safety function, represent an actual loss of safety function for a single train for greater than the Technical Specification allowed outage time, or screen as potentially risk significant due to seismic, fire, flooding, or severe weather initiating events. The finding had a crosscutting aspect in the area of problem identification and Enclosure-5-resolution since Pacific Gas and Electric Company staff failed to adequately trend, assess, and troubleshoot previous Limitorque SMB-000 actuator failures (Section 4OA5.3).

Cornerstone: Barrier Integrity

Green.

An NRC-identified noncited violation of Technical Specification 5.4.1 was identified because Pacific Gas and Electric Company failed to follow the procedure for ensuring that welding preheat temperatures were verified prior to welding. Specifically, during the replacement of Component Cooling Water

Valves 279 and 280, which provide cooling to the reactor vessel support pads,

Pacific Gas and Electric Company failed to verify that the minimum welding preheat temperature of 50°F was met, and could not demonstrate that the ambient temperature was greater than 50°F. Pacific Gas and Electric Company surveyed the area and entered the finding into their corrective action program as

Action Request A0665588.

The finding was greater than minor because it was associated with the human performance attribute of the Barrier Integrity Cornerstone and impacted the cornerstone objective of providing reasonable assurance that physical design barriers, in this case the reactor coolant system, protect the public from radio-

nuclide releases caused by accidents or events. The finding was determined to be of very low safety significance based on management review of the plant conditions at the time the performance deficiency occurred (defueled) and the condition was evaluated prior to the plant entering Mode 5 (Section 1R08).

Cornerstone: Occupational Radiation Safety

Green.

The inspectors identified a noncited violation of 10 CFR 20.1501(a)because Pacific Gas and Electric Company failed to survey to determine the extent and magnitude of radiation levels and evaluate the radiological hazards.

Specifically, on April 18, 2006, the inspectors identified elevated radiation levels near two chemical volume control system valves located in a hallway on the 100-foot elevation of Unit 2. Pacific Gas and Electric Company confirmed elevated radiation levels near the valves were as high as 200 millirem per hour on contact and 28 millirem per hour at 30 centimeters. Pacific Gas and Electric

Company surveyed the area and entered the finding into their corrective action program as Action Request 0665039.

The finding was greater than minor because it was associated with the Occupational Radiation Safety Cornerstone attribute of Exposure Control and

Monitoring and affected the cornerstone objective to ensure the adequate protection of a worker's health and safety from exposure to radiation because workers could have unknowingly received additional radiation exposure. When going through the Occupational Radiation Safety Significance Determination

Process, the finding was determined to be of very low safety significance because it was not an as low as is reasonably achievable finding. There was no overexposure or substantial potential for an overexposure, and the ability to assess dose was not compromised. The finding also had crosscutting aspects Enclosure-6-associated with human performance because adequate resources were not established for the survey requirements (Section 2OS1).

Enclosure-7-

REPORT DETAILS

Summary of Plant Status

Diablo Canyon Unit 1 operated at 100 percent power for this inspection period.

Diablo Canyon Unit 2 began this inspection period at 100 percent power and entered Refueling Outage 2R13 on April 17, 2006. Unit 2 entered Mode 6 (Refueling) for core offload operations

on April 20, which was completed on April 25. Unit 2 entered Mode 6 on May 11 when

operators began reloading fuel into the core, and then entered Mode 5 (Cold Shutdown) on

May 17 when maintenance personnel tensioned the reactor vessel head. Operators

commenced a heatup of the reactor coolant system (RCS), and Unit 2 entered Mode 4 (Hot

Shutdown) on May 21 and Mode 3 (Hot Standby) on May 23. On May 24, operators proceeded

with reactor startup, entering Mode 2 (Startup). Operators increased reactor power, and Unit 2

entered Mode 1 (Power Operations) on May 25. On May 25, Unit 2 was paralleled to the grid, ending Refueling Outage 2R13. On May 26, the operators removed the unit from the grid due

to a seal rub on the low pressure turbine. The main turbine was subsequently paralleled to the

grid on the same day. Operators continued to raise reactor power and, on June 5, Unit 2

reached 100 percent power. On June 21, Unit 2 reduced power to 82 percent to perform

maintenance on high pressure turbine governor Valve FCV-142. Unit 2 was returned to

100 percent power on the same day and remained at that power level for the remainder of the

inspection period.1.REACTOR SAFETY Cornerstones: Initiating Events, Mitigating Systems, and Barrier Integrity1R04Equipment Alignments (71111.04)

.1 Partial System Walkdowns

a. Inspection Scope

The inspectors:

(1) walked down portions of the three below listed risk-important systems and reviewed plant procedures and document s to verify that critical portions of the selected systems were correctly aligned; and
(2) compared deficiencies identified

during the walkdown to the Final Safety Analysis Report (FSAR) Update and corrective

action program (CAP) to ensure problems were being identified and corrected.*April 17, 2006: Unit 2, RCS piping*May 5, 2006: Unit 2, Vital Batteries 2-1, 2-2, and 2-3

  • June 28, 2006: Unit 1, Safety Injection Pump 1-1 Documents reviewed by the inspectors included:
  • Procedure OP B-3A:II, "Safety Injection System Alignment Verification for Plant Startup," Revision 23,*Drawing 106709, "Safety Injection," Sheet 4, Revision 54

-8-The inspectors completed three samples.

b. Findings

No findings of significance were identified.

.2 Complete System Walkdown

a. Inspection Scope

The inspectors:

(1) reviewed plant procedures, calculations, the FSAR Update, Technical Specifications (TSs), and vendor manuals to determine the impact of ultra-low

sulfur diesel fuel on the capability of the diesel engine generators;

(2) reviewed

outstanding design issues, operator workarounds, and FSAR Update documents to

determine if open issues affected the functionality of the diesel engine generators; and

(3) verified that Pacific Gas and Electric Company (PG&E) was identifying and resolving

equipment alignment problems. Documents revi ewed by the inspectors are listed in the attachment.

The inspectors completed one sample.

b. Findings

No findings of significance were identified.

1R05 Fire Protection (71111.05)

.1 Quarterly Inspection

a. Inspection Scope

The inspectors walked down the six below listed plant areas to assess the material condition of active and passive fire protection features and their operational lineup and

readiness. The inspectors:

(1) verified that transient combustibles and hot work

activities were controlled in accordance with plant procedures;

(2) observed the

condition of fire detection devices to verify they remained functional;

(3) observed fire

suppression systems to verify they re mained functional and that access to manual actuators was unobstructed;

(4) verified that fire extinguishers and hose stations were

provided at their designated locations and that they were in a satisfactory condition;

(5) verified that passive fire protection features (electrical raceway barriers, fire doors, fire dampers, steel fire proofing, penetration seals, and oil collection systems) were in a

satisfactory material condition;

(6) verified that adequate compensatory measures were

established for degraded or inoperable fire protection features and that the

compensatory measures were commensurate with the significance of the deficiency; and

(7) reviewed the FSAR Update to determine if PG&E identified and corrected fire

protection problems.*April 10, 2006: Unit 2, 140 foot turbine building

-9-*April 14, 2006: Unit 2, 64 foot auxiliary building*May 1, 2006: Units 1 and 2, intake structure

  • May 2, 2006: Unit 2, Containment Fire Zones 1A, 1B, and 1C
  • May 2, 2006: Unit 1, 85 foot auxiliary building
  • May 8, 2006: Security diesel engine generator building Documents reviewed by the inspectors are listed in the attachment.

The inspectors completed six samples.

b. Findings

No findings of significance were identified.

1R06 Flood Protection Measures (71111.06)

Annual External Flooding

a. Inspection Scope

The inspectors:

(1) reviewed the FSAR Update, the flooding analysis, and plant procedures to assess seasonal susceptibilities involving external flooding;
(2) reviewed

the FSAR Update and CAP to determine if PG&E identified and corrected flooding

problems;

(3) inspected underground bunkers/manholes to verify the adequacy of:
(a) sump pumps,
(b) level alarm circuits,
(c) cable splices subject to submergence, and
(d) drainage for bunkers/manholes;
(4) verified that operator actions for coping with

flooding can reasonably achieve the desired outcomes; and

(5) walked down the one

below listed area to verify the adequacy of:

(a) equipment seals located below the

floodline,

(b) floor and wall penetration seals,
(c) watertight door seals,
(d) common drain

lines and sumps,

(e) sump pumps, level alarms, and control circuits, and
(f) temporary or

removable flood barriers.*April 2, 2006: Units 1 and 2, 500 kV switchyard Pullboxes W-3 and W-4

Documents reviewed by the inspectors are listed in the attachment.

The inspectors completed one sample.

b. Findings

No findings of significance were identified.

1R07 Heat Sink Performance (71111.07)

a. Inspection Scope

The inspectors reviewed PG&E's programs, verified performance against industry standards, and reviewed critical operating parameters and maintenance records for

Component Cooling Water Heat Exchangers 1-1 and 1-2. The inspectors verified that:

-10-(1) performance tests were satisfactorily conducted for heat exchangers/heat sinks and reviewed for problems or errors;

(2) PG&E utilized the periodic maintenance method

outlined in Electric Power Research Institute NP-7552, "Heat Exchanger Performance

Monitoring Guidelines;"

(3) PG&E properly utilized biofouling controls;
(4) PG&E's heat

exchanger inspections adequately assessed the state of cleanliness of their tubes, and

(5) the heat exchanger was correctly categorized under the Maintenance Rule.

Documents reviewed by the inspectors included Procedure PEP -234, "CCW Heat Exchanger Performance Test," Revision 9.

The inspectors completed one sample.

b. Findings

No findings of significance were identified.

1R08 Inservice Inspection Activities (71111.08)

.1 Inspection Activities Other Than Steam Generator Tube Inspections, Pressurized Water

Reactor Vessel Upper Head Penetration Inspections, Boric Acid Corrosion Control

a. Inspection Scope

The procedure requires review of two or three types of nondestructive examination (NDE) activities (volumetric, surface, and visual.) The inspector reviewed multiple examples of all three types.

The procedure requires review of one or two ex aminations from the previous outage with recordable indications that were accepted for continued service. The inspector reviewed

one such examination (Residual Heat Removal System Piping Weld RB-119-II).

If PG&E completed welding on the pressure boundary for Class 1 or 2 systems since the beginning of the previous outage, the procedure requires verification for one-to-three

welds that acceptance and preservice examinations were done in accordance with

American Society of Mechanical Engineers (ASME) Code. The inspector verified one

such weld (Safety Injection System Weld 2SI-119-8III).The procedure requires verification that one or two ASME Section XI Code repairs orreplacements meet Code requirements. The inspector verified two Section XI repairs (replacement of Component Cooling Water Valves 2-279 and 2-280 and replacement of

Residual Heat Removal Valve 2-8742B).

The inspector verified, through direct observation or record review, that ultrasonic, eddy current, liquid penetrant, radiographic, or visual examinations of the components listed

below were performed in accordance with ASME Code requirements.

-11-System Component/Weld Identification Examination MethodFeedwaterSteam Generator 1 Feedwater Supply Hanger 2037-7V Visual (VT-3)

Auxiliary Feedwater (AFW)

AFW Pump 2-1 Discharge Header Hanger 414-505R Visual (VT-3)AFWAFW Pump 2-1 Discharge Header Hanger 414-386R Visual (VT-3)AFWAFW Supply Hanger 42-42RVisual (VT-3)

Chemical Volume Control SystemCVCS-2-8388C, FW-2RadiographicFeedwaterK16-555-16/Integral AttachmentsMagnetic Particle &

UltrasonicFeedwaterK16-557-16Magnetic Particle &

UltrasonicReactor CoolantS6-959-2 SPL WIB-503Liquid Penetrant Reactor CoolantS6-959-2 SPL WIB-1009Liquid Penetrant Reactor VesselCircumferential Weld 9-201Ultrasonic Reactor VesselLoop 2 Outlet Safe-endUltrasonic During the review of each examination, the inspector verified that the correct NDE procedures were used, that examinations and conditions were as specified in the

procedure, and that test instrumentation or equipment was properly calibrated and within

the allowable calibration period. The inspector also reviewed documentation such as

ultrasonic and eddy current inspection records to determine if the indications revealed by

the examinations were compared against the ASME Code specified acceptance

standards. This review also determined that indications were appropriately

dispositioned.

The inspector verified the NDE certifications of those personnel observed performing examinations or identified during review of completed examination packages.

The inspector also reviewed the replacement of four valves performed in accordancewith ASME Section XI. During the replacement of two component cooling water valves

-12-that supply cooling to the reactor vessel support pads, the inspector found that PG&E did not verify the minimum preheat temperature prior to welding.

The minimum sample requirements of the inspection procedure were satisfied.

b. Findings

Introduction

A Green, noncited violation (NCV) of TS 5.4.1.a was identified for failure to follow the procedure for ensuring that welding preheat temperatures were verified prior

to welding. Specifically, on April 26, 2006, during the replacement of Component

Cooling Water Valves 279 and 280, which provide cooling to the reactor vessel support

pads, PG&E failed to verify that the minimum welding preheat temperature of 50°F was

met and PG&E could not demonstrate that the ambient temperature was greater than

50°F. Description

The replacement of Valves 279 and 280 was performed in accordance with Work Order CO196956, which referenced Welding Procedure Specification 5, "Welding

of P1 Materials with GTAW and/or SMAW," Revision 8; Nuclear Welding Control Manual

Procedures GWS-ASME,"ASME General Welding Standard," Revision 8; and WI-1, "Visual Inspection of Welds," Revision 7. Welding Procedure Specification 5 lists a

minimum preheat temperature of 50°F as an essential variable. Section 4.5 of

GWS-ASME states that preheat temperature shall be verified with thermocouples or

temperature indicating crayons or contact pyrometers outside the weld joint but near the

weld area. Section 6.7 of Procedure WI-1 states that verification of preheat temperature

is not mandatory for welds that require a minimum preheat of 50°F, if it can be

demonstrated that the ambient temperature is greater than 50°F. During the

replacement of Valves 279 and 280, PG&E did not verify the preheat temperature prior

to welding. The containment building was open to the environment and no ambient

temperature measurement was performed to demonstrate that the ambient temperature was greater than 50°F.

Analysis:

The performance deficiency associated with this finding is a failure to follow procedures. This deficiency impacted the Barrier Integrity Cornerstone and, as

described in Inspection Manual Chapter (IMC) 0612, Appendix B, the finding was

considered more than minor since it affected the cornerstone objective of providing

reasonable assurance that physical design barriers, in this case the RCS, protect the

public from radionuclide releases caused by a ccidents or events. Specifically, the failure to ensure minimum preheat temperature prior to welding affected the cornerstone

attribute of human performance and its impact on maintaining functionality of the RCS

because not adequately controlling the welding process can lead to weld failures.

Minimum preheat temperature is defined in Section IX of the ASME Code as an

essential variable which can affect the mechanical properties of a weldment. For carbon

steels or low alloy steels, the failure to observe the specified minimum preheat

temperature could result in too rapid cooling and the formation of martensite, a brittle

structure. Rapid cooling could also impede the ability of the weldment to evolve gases

introduced or formed during the welding operation, leading to hydrogen embrittlement.

The finding was determined to be of very low safety significance based on management

review of the plant conditions at the time the performance deficiency occurred (defueled)

and the condition was evaluated prior to the plant entering Mode 5.

-13-Enforcement

TS 5.4.1.a requires that written procedures shall be established, implemented, and maintained covering the applicable procedures recommended in

Appendix A of Regulatory Guide 1.33, Revision 2, Appendix A, February 1978.

Appendix A, Section 9, lists procedures for performing maintenance activities, such as

welding. Welding Procedure Specification 5 and Nuclear Welding Control Manual

Procedures GWS-ASME and WI-1 require that minimum preheat temperature be verified

prior to welding. Contrary to the above, on April 24, 2006, PG&E failed to follow these

procedures by not verifying the preheat tem perature nor that the ambient temperature was above 50°F before beginning welding on Component Cooling Water Valves 279

and 280. Because the failure to follow procedures was of very low safety significance

and has been entered into the CAP as Action Request (AR) A0665588, this violation is

being treated as an noncited violation, consistent with Section VI.A of the NRC

Enforcement Policy: NCV 50-323/06-03-01, Failure to Follow Procedures for Welding.

.2 Pressurized Water Reactor Vessel Upper Head Penetration Inspection Activities

a. Inspection Scope

The inspector reviewed PG&E's reactor vessel upper head penetration (VUHP) nozzle inspection activities implemented in accordance with the requirements of NRC

Order EA-03-009, issued on February 20, 2004. PG&E's nonvisual NDE technique was

a surface examination using ultrasonic and eddy current testing of the wetted surface of

the VUHP nozzle base material and the J-groove weld.

The inspector observed a sample of NDE performed on the vessel head from remote video feeds at the collection and analysis stations. The inspector examined ultrasonic

and eddy current data collected. A review of the NDE examination procedures used was

also performed to confirm that they were consistent with the ASME Code and that the

equipment and calibration requirements were consistent with that used in mockup

demonstrations on simulated actual cracking. The inspector also reviewed records

indicating the extent of inspection for each penetration nozzle, including documents

which resolved interference or masking issues. Specifically, the inspector verified that

PG&E achieved ultrasonic testing coverage to the maximum extent possible. In all

cases, the coverage was from 2 inches above the J-groove weld down to the lowest

elevation that could be practically inspected on each nozzle with the ultrasonic testing

probe being used with a minimum required inspection distance of 0.3 inches below the

J-groove weld. This criteria was specified in an NRC approved alternate examination

criteria for 78 VUHP nozzles.

For all activities reviewed, the inspector determined that the activities were performed in accordance with the requirements of the NRC Order. No indications or defects were

detected. There had not been any indications previously identified which had been

accepted for continued service.

The minimum sample requirements of the inspection procedure were satisfied.

b. Findings

No findings of significance were identified.

-14-

.3 Boric Acid Corrosion Control Inspection Activities (Pressurized Water Reactors)

a. Inspection Scope

The inspector reviewed a sample of boric acid corrosion control walkdown visual examination activities. The inspector determined that PG&E's visual inspections

emphasized locations where boric acid leaks could cause degradation of safety

significant components.

The inspector reviewed three engineering evaluations performed for boric acid found on RCS piping and components. The review verified that ASME Code wall thickness

requirements were maintained and that the degraded conditions were properly entered

and dispositioned in PG&E's CAP.

The minimum sample requirements of the inspection procedure were satisfied.

b. Findings

No findings of significance were identified.

.4 Steam Generator Tube Inspection Activities

a. Inspection Scope

The inspector verified that the steam generator tube eddy current examination scope and expansion criteria met the TS requirements, industry guidelines, and commitments

made to the NRC. The inspector confirmed that known areas of potential degradation

based on site-specific and industry experience were included in the scope of the

inspection. The inspector observed the collection and analysis of eddy current data by

contractor personnel and verified that:

(1) the eddy current probes being utilized were

appropriate for identifying the expected types of indications,

(2) probe position location

verification was being performed,

(3) calibration requirements were being adhered to, and
(4) probe travel speed was in accordance with procedural requirements.

The inspector verified that PG&E compared flaws detected during the current outage against the previous outage data and that appropriate repair criteria was specified. One

hundred percent of all steam generator tubes were inspected during this outage. The

inspector noted that the number of tubes required to be plugged was consistent with

predictions made prior to the start of the outage. Tube plugging activities during the

inspection were in accordance with procedural requirements and were within the

allowable limits for tube plugging.

The minimum sample requirements of the inspection procedure were satisfied.

b. Findings

No findings of significance were identified.

1R11 Licensed Operator Requalification (71111.11)

-15-

.1 Quarterly Inspection

a. Inspection Scope

The inspectors observed testing and training of senior reactor operators and reactor operators to identify deficiencies and discrepancies in the training, to assess operator

performance, and to assess the evaluator's critique. The training scenario involved a

positive displacement pump overcurrent trip , loss of a vital 4 kV bus, an earthquake, and an anticipated transient without scram.

Documents reviewed by the inspectors included Lesson FRS1-A, Attachment 2,"Simulator Event Sequence," Revision 14.

The inspectors completed one sample.

b. Findings

No findings of significance were identified.

.2 Biennial Inspection

a. Inspection Scope

Following the completion of the annual operating examination testing cycle, which ended the week of April 4, 2006, the inspectors reviewed the overall pass/fail results of the

annual individual job performance measure operating tests and simulator operating tests

administered by PG&E staff during the operator licensing requalification cycle. Sixteen

separate crews participated in simulator operating tests, and 79 licensed operators took

the job performance measure operating tests. All of the crews tested passed the

simulator portion of the annual operating test. All of the licensed operators, except one, passed the job performance measure portion of the examination. The licensed operator

was successfully remediated prior to returning to shift. These results were compared to

the thresholds established in IMC 609, Appendix I, "Operator Requalification Human

Performance Significance Determination Process." The inspectors completed one sample.

b. Findings

No findings of significance were identified.

1R12 Maintenance Effectiveness (71111.12)

a. Inspection Scope

The inspectors reviewed the one below listed maintenance activity to:

(1) verify the appropriate handling of structure, system, and component (SSC) performance or

condition problems;

(2) verify the appropriate handling of degraded SSC functional

performance;

(3) evaluate the role of work practices and common cause problems; and

-16-(4) evaluate the handling of SSC issues reviewed under the requirements of the Maintenance Rule, 10 CFR Part 50, Appendix B, and the TSs.*May 1, 2006: Units 1 and 2, Containment isolation valves

Documents reviewed by the inspectors are listed in the attachment.

The inspectors completed one sample.

b. Findings

No findings of significance were identified.

1R13 Maintenance Risk Assessments and Emergent Work Control (71111.13)

.1 Risk Assessments and Management of Risk

a. Inspection Scope

The inspectors reviewed the one below listed assessment activities to verify:

(1) performance of risk assessments when required by 10 CFR 50.65(a)(4) and PG&E

procedures prior to changes in plant configuration for maintenance activities and plant

operations;

(2) the accuracy, adequacy, and completeness of the information considered

in the risk assessment;

(3) that PG&E recognizes, and/or enters as applicable, the

appropriate risk category according to the risk assessment results and PG&E

procedures; and

(4) that PG&E identified and corrected problems related to maintenance risk assessments.*April 5, 2006: Unit 2; Diesel Fuel Oil Transfer Pump 0-1 and Electrohydraulic Pump 2-2 preventive maintenance, 500 kV Circuit Breaker 542 replacement, and

Morro Bay to Diablo Canyon 230 kV line outage due to fiber optic cable

installation.

Documents reviewed by the inspectors included Procedure AD7.DC6, "On-line Maintenance Risk Management," Revision 9.

The inspectors completed one sample.

b. Findings

No findings of significance were identified.

.2 Emergent Work

a. Inspection Scope

The inspectors:

(1) verified that PG&E performed actions to minimize the probability of initiating events and maintained the functional capability of mitigating systems and

barrier integrity systems;

(2) verified that emergent work-related activities such as

-17-troubleshooting, work planning/scheduling, establishing plant conditions, aligning equipment, tagging, temporary modifications, and equipment restoration did not place

the plant in an unacceptable configuration; and

(3) reviewed the FSAR Update to

determine if PG&E identified and corrected risk assessment and emergent work control

problems.*April 2, 2006: Unit 1, Diesel Engine Generator 1-3 voltage regulator failure

  • June 3, 2006: Unit 1, Failure of rod control system to manually withdraw Bank D control rods from core Documents reviewed by the inspectors are listed in the attachment.

The inspectors completed two samples.

b. Findings

No findings of significance were identified.

1R14 Personnel Performance Related to Nonroutine Plant Evolutions and Events (71111.14)

a. Inspection Scope

The inspectors:

(1) reviewed operator logs, plant computer data, and/or strip charts for the below listed evolutions to evaluate operator performance in coping with nonroutine

events and transients;

(2) verified that operator actions were in accordance with the

response required by plant procedures and training; and

(3) verified that PG&E has

identified and implemented appropriate corrective actions associated with personnel

performance problems that occurred during the nonroutine evolutions sampled.*April 23, 2006: Unit 2, Fuel handling cart position resolver failed while a fuelassembly was in motion*May 4, 2006: Units 1 and 2, Magnitude 2.8 earthquake approximately 6 km west northwest of Diablo Canyon Power Plant*May 25, 2006: Unit 2, Auxiliary Transformer 2-1 sudden pressure trip

Documents reviewed by the inspectors are listed in the attachment.

The inspectors completed three samples.

b. Findings

No findings of significance were identified.

1R15 Operability Evaluations (71111.15)

a. Inspection Scope

-18-The inspectors:

(1) reviewed plant status documents, such as operator shift logs, emergent work documentation, deferred modifications, and standing orders, to

determine if an operability evaluation was warranted for degraded components;

(2) referred to the FSAR Update and design bases documents to review the technical

adequacy of the operability evaluations;

(3) evaluated compensatory measures

associated with operability evaluations;

(4) determined degraded component impact on

any TS;

(5) used the significance determination process to evaluate the risk significance

of degraded or inoperable equipment; and

(5) verified that PG&E has identified and

implemented appropriate corrective actions associated with degraded components.*April 14, 2006: Unit 1, Condensate storage tank epoxy delamination*April 14, 2006: Unit 2, Residual heat removal system weld flaw

  • May 8, 2006: Unit 2, Station vital inverters
  • May 9, 2006: Units 1 and 2, Feedwater ultrasonic flow meter data scatter
  • May 21, 2006: Unit 2, Accumulator 2-3 discharge line water hammer Documents reviewed by the inspectors are listed in the attachment.

The inspectors completed five samples.

b. Findings

Introduction:

A self-revealing, NCV of 10 CFR Part 50, Appendix B, Criterion XVI, was determined for the failure of operators to promptly identify a condition adverse to quality.

Specifically, operators failed to document in the CAP an unexpected level drop in

Accumulator 1-3 during Refueling Outage 1R13. Failure to enter the occurrence into the

CAP precluded corrective actions that would have prevented the unexpected level drop

in Accumulator 2-3 and the water hammer of its discharge piping.

Description

On May 21, 2006, with Unit 2 in Mode 4 and reactor coolant system pressure at 935 psig, operators opened Accumulator 2-3 Discharge Valve SI-2-8808C

and subsequently Accumulator 2-3 level unexpectedly dropped from 67 to 57 percent.

At the same time, operators received a Reactor Coolant Pump 2-3 vibration alarm and

audible indications of a water hammer from inside containment. PG&E staff concluded

that a water hammer had occurred inside the discharge piping of Accumulator 2-3. As

immediate corrective actions, PG&E staff visually walked down Accumulator 2-3

discharge piping and supports, verified operability of the discharge piping seismic

snubbers, and verified the absence of voids in other portions of Units 1 and 2 emergency

core cooling system piping. Upon review of Accumulator 2-3 piping layout, PG&E staff

found that there were no vent points in the accumulator discharge piping between motor-

operated discharge Valve SI-2-8808C and discharge check Valve SI-2-8956C.

Additionally, there were no procedures that specifically addressed the venting of the

discharge line. The inspectors calculated approximately 83 feet of 10-inch pipe between

the two valves, which equated to an approximate volume of 34.7 ft

3. PG&E initiated a

root cause investigation under Nonconformance Report N0002207 to determine the

cause(s) and appropriate corrective actions for the water hammer event.

-19-While investigating the cause of the water hammer event, PG&E staff learned that a similar event had occurred with Accumulator 1-3 during Refueling Outage 1R13. On

November 27, 2005, operators opened Accumulator 1-3 Discharge Valve SI-1-8808C

and observed an approximate 7 percent level drop in the accumulator. However, there

were no corresponding indications of a water hammer, such as an audible noise or

reactor coolant pump vibration alarms. Although the level drop was recorded in the

operator logs, operators failed to enter the unexpected occurrence into the CAP. PG&E

staff has since entered the occurrence as AR A0669453.

The inspectors determined that the failure to address the Unit 1 accumulator level drop precluded corrective actions from being taken to prevent a recurrence of the event on

Unit 2. Specifically, PG&E staff should have identified the voided condition after the

Unit 1 accumulator level drop and that there was potential for voiding of the accumulator

discharge piping due to the absence of vent points and procedures for venting.

Analysis:

The performance deficiency associated with this finding involved a failure of operations personnel to promptly identify a condition adverse to quality and enter it into

the CAP. The performance deficiency was self-revealing based on the second event

initiating the licensee's review of the cause and subsequent identification that the event

had occurred on Unit 1 also. The finding is greater than minor because it is associated

with the Mitigating Systems Cornerstone attribute of configuration control and affects the

associated cornerstone objective to ensure the availability, reliability, and capability of

systems that respond to initiating events to prevent undesirable consequences. Using

the IMC 0609, "Significance Determination Process," Appendix A, Phase 1 Screening

Worksheet, the finding is determined to be of very low safety significance because the

finding did not represent a loss of safety function, an actual loss of a safety-related train

for greater than its TS allowed outage time, or screen as potentially risk-significant due

to seismic, fire, flooding, or severe weather initiating events. The finding had a

crosscutting aspect in the area of problem identification and resolution because

operations personnel failed to promptly identify, in the CAP, the unexpected level drop in

Accumulator 1-3.

Enforcement:

10 CFR Part 50, Appendix B, Criterion XVI, "Corrective Action," requires, in part, that measures be established to assure that conditions adverse to quality are

promptly identified and corrected. Contrary to this, between November 27, 2005, and

May 24, 2006, operations personnel failed to assure that a condition adverse to quality

was promptly identified. Specifically, on November 27, 2005, the level in

Accumulator 1-3 unexpectedly dropped 7 percent when operators opened its discharge

valve. Although operators documented the event in their logs, they failed to enter the

occurrence into the CAP. Subsequently, no corrective actions were taken. On

May 21, 2006, when the discharge valve on Accumulator 2-3 was opened, its level

unexpectedly dropped by 10 percent and a water hammer occurred in its discharge

piping. The apparent cause of the failure to promptly identify a condition adverse to

quality was that operators did not recognize the significance of the Accumulator 1-3 level

drop. Corrective actions include additional training of operations personnel regarding

the importance of promptly identifying conditions adverse to quality. Because the finding

is of very low safety significance and has been entered into PG&E's CAP as

AR A0669468, this violation is being treated as an NCV consistent with Section VI.A of

-20-the Enforcement Policy: NCV 50-275/06-03-02, Failure to Promptly Identify Voiding in Accumulator Discharge Line.

1R17 Permanent Plant Modifications (71111.17)

a. Inspection Scope

The inspectors reviewed key affected parameters associated with energy needs, materials/replacement components, timing, heat removal, control signals, equipment

protection from hazards, operations, flowpaths, pressure boundary, ventilation boundary, structural, process medium properties, licensing basis, and failure modes for the one

modification listed below. The inspectors verified that:

(1) modification preparation, staging, and implementation did not impair emergency/abnormal operating procedure

actions, key safety functions, or operator response to loss of key safety functions;

(2) postmodification testing maintained the plant in a safe configuration during testing by

verifying that unintended system interactions will not occur, SSC performance

characteristics still met the design basis, the appropriateness of modification design

assumptions, and the modification test acceptance criteria has been met; and

(3) PG&E

has identified and implemented appropriate corrective actions associated with

permanent plant modifications. *May 19, 2006: Removal of mesh over the residual heat removal suction point in the containment recirculation sump and modifications to the reactor cavity door to

address recirculation sump debris loading concerns Documents reviewed by the inspectors are listed in the attachment.

The inspectors completed one sample.

b. Findings

No findings of significance were identified.

1R19 Postmaintenance Testing (71111.19)

a. Inspection Scope

The inspectors selected the nine below listed postmaintenance test activities of risk-significant systems or components. For each item, the inspectors:

(1) reviewed the

applicable licensing basis and/or design basis documents to determine the safety

functions;

(2) evaluated the safety functions that may have been affected by the

maintenance activity; and

(3) reviewed the test procedure to ensure it adequately tested

the safety function that may have been affected. The inspectors either witnessed or

reviewed test data to verify that acceptance criteria were met, plant impacts were

evaluated, test equipment was calibrated, procedures were followed, jumpers were

properly controlled, the test data results were complete and accurate, the test equipment

was removed, the system was properly realigned, and deficiencies during testing were

documented. The inspectors also reviewed the FSAR Update to determine if PG&E

identified and corrected problems related to postmaintenance testing.

-21-*April 18, 2006: Unit 2, Containment Spray Pump 2-1 and 2-2*April 20, 2006: Unit 2, Source Range Nuclear Instrument 31

  • May 2, 2006: Unit 2, Component Cooling Water Pump 2-3
  • May 2, 2006: Unit 2, Vital Inverter IY-21
  • May 2, 2006: Unit 2, 4kV Vital Bus "H" Switchgear
  • May 5, 2006: Unit 2, Auxiliary Saltwater Pump 2-2
  • May 11, 2006: Unit 2, Centrifugal Charging Pump 2-1
  • May 12, 2006: Unit 2, Fuel transfer cart position resolver
  • May 18, 2006: Unit 2, Auxiliary Transformer 2-1 Documents reviewed by the inspectors are listed in the attachment.

The inspectors completed nine samples.

b. Findings

No findings of significance were identified.

1R20 Refueling and Outage Activities (71111.20)

a. Inspection Scope

The inspectors reviewed the following risk-significant refueling items or outage activities to verify defense-in-depth commensurate with the outage risk control plan, compliance

with the TS, and adherence to commitments in response to Generic Letter 88-17, "Loss

of Decay Heat Removal":

(1) the risk control plan;
(2) tagging/clearance activities;
(3) RCS instrumentation;
(4) electrical power;
(5) decay heat removal;
(6) spent fuel pool

cooling;

(7) inventory control;
(8) reactivity control;
(9) containment closure;
(10) reduced

inventory or midloop conditions;

(11) refueling activities;
(12) heatup and cooldown

activities;

(13) restart activities; and
(14) identification and implementation of appropriate

corrective actions associated with refueling and outage activities. The inspectors'

containment inspections included observations of the containment sump for damage and

debris and supports, braces, and snubbers for evidence of excessive stress, water

hammer, or aging. Documents reviewed by the inspectors included the Unit 2 Refueling

Outage 2R13 Outage Safety Plan.

The inspectors completed one sample.

b. Findings

Introduction

An NRC-identified NCV of TS 5.4.1.a was determined for an inadequate procedure, Procedure OP A-2:II, "Reactor Vessel - Draining the RCS to the Vessel

Flange - With Fuel in Vessel," Revision 33A. Specifically, the procedure did not address

the reactor vessel level instrumentation required by the procedure deviated from actual

level by approximately 15 inches when the time to boiling in the reactor vessel was

approximately 20 minutes, if shutdown cooling were lost.

-22-Description

One action to ensure the integrity of shutdown cooling by operators was to prevent reactor vessel water level from dropping below the 107.5 foot elevation, where

vortexing of the shutdown cooling pumps may occur. To monitor reactor vessel water

level, operators used three RCS water level instruments when above 112 foot elevation.

The first level instrument was the wide-range reactor vessel refueling level instrument

system (RVRLIS), which consisted of two pressure transmitters measuring the

differential pressure across the RCS. The reference leg transmitter was located at the

top of the pressurizer and the variable leg transmitter was located at the Loop 4

crossover leg. The second level instrument was LI-400, which is a clear standpipe with

internal flags that indicate water level. LI-400 had essentially the same range and

instrument tap locations as wide-range RVRLIS. The third level instrument was the

narrow-range RVRLIS, which also consisted of two pressure transmitters that measured

the differential pressure across the upper portion of the reactor vessel. The reference

leg transmitter was located at the reactor head vent, and the variable leg transmitter was

located at the Loop 3 hot leg.

On April 20, 2006, in preparation for reactor vessel head removal, operators lowered water level in the reactor vessel to the 112 foot elevation (2 feet below the vessel flange)

using Procedure OP A-2:II. At the 112 foot elevation, the time for water in the reactor

vessel to boil, if shutdown cooling were lost, was reduced to approximately 20 minutes.

During the RCS draindown to the 112 foot elevation, Procedure OP A-2:II required

operators to maintain wide-range RVRLIS and LI-400 level indications in agreement by

+/- 9 inches. However, Procedure OP A-2:II did not require the instruments to agree

once level reached the 112 foot elevation. Additionally, Procedure OP A-2:II allowed

operators to place into service narrow-range RVRLIS and required it to read within

+/- 4 inches of LI-400 initially, but not for the duration of the RCS depressurization which

was to follow.

Once operators reached the 112 foot elevation and placed narrow-range RVRLIS in service, they began to depressurize the RCS according to Procedure OP A-2:II. During

the depressurization, operators observed that both required instruments, wide-range

RVRLIS and LI-400 began to show increasing level, while the optional narrow-range

RVRLIS water level remained stable at 112 feet. The deviation between narrow-range

RVRLIS and the other two instruments grew to approximately 15 inches before levels

stabilized. PG&E staff determined that a pressure differential existed between the gas

spaces of the pressurizer and reactor vessel. The RCS was depressurized via the

pressurizer relief tank with an approximate 1-inch outer diameter pipe. The

communication path between the pressurizer and reactor vessel gas spaces was also an

approximate 1-inch outer diameter pipe.

Despite the communication pathway, the depressurization activities would cause the pressurizer gas space to have a lower

pressure than the reactor vessel gas space. Subsequently, the wide-range RVRLIS and

LI-400 instruments would read lower (reference from the pressurizer gas space) than

narrow-range RVRLIS (referenced from the reactor vessel gas space).

The inspectors reviewed operating experience from both the Diablo Canyon Power Plant and the nuclear industry. Specifically, the inspectors reviewed Generic Letter 88-17, "Loss of Decay Heat Removal." Generic Letter 88-17 specifically addressed reduced

inventory evolutions, which is defined as 3 feet below the reactor vessel flange. While

the evolution on April 20, 2006, involved an RCS level that was only 2 feet below the

-23-reactor vessel flange, the time-to-boiling estimate was short (approximately 20 minutes).

Therefore, the inspectors determined that many of the recommendations in Generic

Letter 88-17 could be considered as operating experience for this evolution. An example

of a recommendation was the consideration of various phenomena that could affect level

instrumentation, including the inability of gas spaces to communicate if the RCS legs are

full of water. Also, Generic Letter 88-17 recommended reliable, accurate RCS water

level information for operators whenever approaching or operating in a condition where a

loss of level can lead to loss of decay heat removal. Through discussions with operators

and a review of Procedure OP A-2:II, the inspectors observed that Diablo Canyon Power

Plant had operating experience that would demonstrate that the level instrumentation

would tend to deviate when the RCS was being depressurzied.

The inspectors determined that PG&E staff had failed to adequately maintain Procedure OP A-2:II. First, wide-range RVRLIS and LI-400 were the required RCS level

instruments during the RCS depressurization at the 112 foot elevation, even though

these instruments would tend to read nonconservatively due to the pressure differences

in the gas spaces of the pressurizer and the reactor vessel. The inspectors determined

that an adequate review of operating experience would have demonstrated that these

level instruments were nonconservative for the depressurization evolution. Second, Procedure OP A-2:II did not have criteria regarding the performance of the RCS level

instruments during the RCS depressurization evolution. Although operators knew that

RCS level instruments may deviate from each other during the depressurization, there

was no criteria that would have given operators information that abnormal level

deviations were occurring and may be indicative of unexpected equipment operation, problems, or phenomenon. Generic Letter 88-17 had recommended that licensees

consider various phenomenon that could affect level instrumentation and that reliable

and accurate RCS level information be provided to the operator to the extent possible

when approaching conditions that could challenge loss of decay heat removal.

Analysis:

The performance deficiency associated with this finding involved the failure to maintain Procedure OP A-2:II. The finding is greater than minor because it is associated

with the Mitigating Systems Cornerstone attribute of procedure quality and affects the

associated cornerstone objective to ensure the availability, reliability, and capability of

systems that respond to initiating events to prevent undesirable consequences. Using

IMC 0609, Appendix G, Attachment 1, Checklist 3, the finding is determined to be of very

low safety significance since one set of instrumentation provided accurate RCS level

indication and there was no loss of RCS inventory control. The finding had a crosscutting aspect in the area of human performance for resources because PG&E

failed to ensure the adequacy of the procedures used for reactor vessel level monitoring

to ensure nuclear safety.

Enforcement

TS 5.4.1.a requires that written procedures be established, implemented, and maintained covering the activities specif ied in Appendix A, "Typical Procedures for Pressurized Water Reactors and Boiling Water Reactors," of Regulatory Guide 1.33, "Quality Assurance Program Requirements (Operation)," dated February 1978.

Regulatory Guide 1.33, Appendix A, Section 2, requires procedures for refueling

operations. Contrary to this, Procedure OP A-2:II, "Reactor Vessel - Draining the RCS

to the Vessel Flange - With Fuel in Vessel," was inadequate because the procedures

required the wide-range RVRLIS and LI-400 to be in service during RCS

-24-depressurization, despite operating experience that demonstrated these instruments would read nonconservatively. Additionally, Procedure OP A-2:II did not have criteria

that alerted operators to abnormal level instrument deviations that may be caused by

phenomena outside of the level deviations expected by the RCS depressurization.

PG&E has planned to evaluate potential changes to Procedure OP A-2:II and RCS water

level instrumentation when used during RCS depressurization. Because the finding is of

very low safety significance and has been entered into PG&E's CAP as ARs A0664484, A0672419, and A0672422, this violation is being treated as an NCV consistent with

Section VI.A of the Enforcement Policy: NCV 50-323/06-03-03, Inadequate Refueling

Procedure for Draining and Depressurizing the Reactor Coolant System.

1R22 Surveillance Testing (71111.22)

a. Inspection Scope

The inspectors reviewed the FSAR Update, procedure requirements, and TS to ensure that the six below listed surveillance activities demonstrated that the SSC's tested were

capable of performing their intended safety functions. The inspectors either witnessed

or reviewed test data to verify that the following significant surveillance test attributes

were adequate:

(1) preconditioning;
(2) evaluation of testing impact on the plant;
(3) acceptance criteria;
(4) test equipment;
(5) procedures;
(6) jumpers;
(7) test data;
(8) testing frequency and method demonstrated TS operability;
(9) test equipment

removal;

(10) restoration of plant system s;
(11) fulfillment of ASME Code requirements;
(12) updating of performance indicator (PI) data;
(13) engineering evaluations, root

causes, and bases for returning tested SSCs not meeting the test acceptance criteria

were correct;

(14) reference setting data; and
(15) annunciators and alarm setpoints.

The inspectors also verified that PG&E identified and implemented any needed

corrective actions associated with the surveillance testing.*April 17, 2006: Unit 1, Procedure STP M-9I, "Diesel Generator Start and Load Tracking," Revision 19, and STP M-9A, "Diesel Engine Generator Routine

Surveillance Test," Revision 70*April 19, 2006: Unit 2, Procedures STP P-CSP-A22, "Comprehensive Testing of Containment Spray Pump 2-2," Revision 2 and STP P-CSP-A21, "Comprehensive Testing of Containment Spray Pump 2-1," Revision 1*May 1, 2006: Unit 2, Procedure STP 102, "Test of Backup Nitrogen Accumulator System to Spray Valves and Charging Valves 8145, 8146, and 8147,"

Revision 23*May 8, 2006: Unit 2, Procedure STP MP-I-7-T411H, "Control Bank D Rod Position Indication and Rod Stop C-11 Calibration," Revision 5A*May 8, 2006: Units 1 and 2, Procedure SP-312, "Security System Emergency Power Source and Load Transferring System," Revision 15B*May 16, 2006: Unit 2, Procedure STP 15, "Integrated Test of Engineered Safeguards and Diesel Generators," Revision 38A

-25-The inspectors completed six samples.

b. Findings

No findings of significance were identified.

===Cornerstone: Emergency Preparedness1EP4Emergency Action Level and Emergency Plan Changes (71114.04)

a. Inspection Scope

=

The inspectors performed in-office reviews of Revision 4, Change 5 to Section 4 of the Diablo Canyon, Units 1 and 2, Emergency Plan, and Revision 34 to Emergency Plan

Implementing Procedure EP G-1, "Emergency Classification and Emergency Plan

Activation," both submitted in February 2006.

These revisions changed emergency classification level descriptions and revised emergency action levels as described in NRC Bulletin 2005-002, "Emergency

Preparedness and Response Actions for Security-Based Events." These revisions were compared to their previous revisions, to the criteria of NUREG-0654, "Criteria for Preparation and Evaluation of Radiological Emergency

Response Plans and Preparedness in Support of Nuclear Power Plants," Revision 1; to

Nuclear Energy Institute (NEI) 99-01, "Methodology for Development of Emergency Action Levels," Revision 2; to NRC Bulletin 2005-02, and to the requirements of

10 CFR 50.47(b) and 50.54(q), to determine if PG&E adequately implemented

10 CFR 50.54(q).

This review was not documented in a Safety Evaluation Report and did not constitute the approval of licensee changes; therefore, these changes are subject to future inspection.

The inspectors completed two samples during this inspection.

b. Findings

No findings of significance were identified.1EP6Emergency Preparedness Evaluation (71114.06)

a. Inspection Scope

For drills contributing to drill/exercise performance and Emergency Response Organization PIs, the inspectors:

(1) observed the training evolution to identify any

weaknesses and deficiencies in classification, notification, and protective action

recommendation development activities;

(2) compared the identified weaknesses and

deficiencies against PG&E identified findings to determine whether PG&E is properly

identifying failures; and

(3) determined whether PG&E performance is in accordance

-26-with the guidance of the NEI 99-02, "Voluntary Submission of Performance Indicator Data," acceptance criteria.*June 1, 2006: A full drill involving a main steam line break, a steam generator tube rupture, and failed fuel cladding, including the turnover between two

emergency response organization crews*June 9, 2006: A simulator-based drill involving a main steam line break where a PI opportunity for classification of Notice of Unusual Event 28 existed Documents reviewed by the inspectors included the Diablo Canyon Power Plant Emergency Plan, Revision 4, and Lesson R061S5, "Imminent PTS," Revision 0.

The inspectors completed two samples.

b. Findings

No findings of significance were identified.2.RADIATION SAFETY

===Cornerstone: Occupational Radiation Safety2OS1Access Control to Radiologically Significant Areas (71121.01)

a. Inspection Scope

=

This area was inspected to assess PG&E's performance in implementing physical and administrative controls for airborne radioactivity areas, radiation areas, high radiation

areas, and worker adherence to these controls. The inspectors used the requirements

in 10 CFR Part 20, the TSs, and PG&E's procedures required by TSs as criteria for

determining compliance. During the inspection, the inspectors interviewed the radiation

protection manager, radiation protection supervisors, and radiation workers. The

inspectors performed independent radiation dose rate measurements and reviewed the

following items:*PI events and associated documentation packages reported by PG&E in the Occupational Radiation Safety Cornerstone *Controls (surveys, posting, and barricades) of radiation, high radiation, and airborne radioactivity areas *Radiation work permits, procedures, engineering controls, and air sampler locations *Conformity of electronic personal dosimeter alarm setpoints with survey indications and plant policy, and workers' knowledge of required actions when

their electronic personnel dosimeter noticeably malfunctions or alarms

-27-*Barrier integrity and performance of engineering controls in airborne radioactivity areas*Physical and programmatic controls for highly activated or contaminated materials (nonfuel) stored within spent fuel and other storage pools*Self-assessments, audits, licensee event reports, and special reports related to the access control program since the last inspection *Corrective action documents related to access controls

  • Radiation work permit briefings and worker instructions
  • Adequacy of radiological controls such as required surveys, radiation protection job coverage, and contamination controls during job performance*Dosimetry placement in high radiation work areas with significant dose rate gradients*Changes in licensee procedural controls of high dose rate - high radiation areas and very high radiation areas*Controls for special areas that have the potential to become very high radiation areas during certain plant operations*Posting and locking of entrances to all accessible high dose rate - high radiation areas and very high radiation areas*Radiation worker and radiation protection technician performance with respect to radiation protection work requirements The inspectors completed 19 samples.

b. Findings

Introduction

The inspectors identified a noncited violation of 10 CFR 20.1501(a)because PG&E failed to perform a survey to identify the magnitude and extent of radiation levels for radiological hazards. The violation had very low safety significance.

Description

On April 18, 2006, the inspectors toured the 100-foot elevation of the Unit 2 auxiliary building and identified elevated radiat ion levels near Chemical Volume Control System Valves CVCS-2-8502 and CVCS-2

-8512A. Subsequent surveys by PG&E confirmed radiation levels of up to 200 millirem per hour on contact and 28 millirem per hour at 30 centimeters in this area. From a review of a previous survey map, the inspectors noted that the highest general area radiation level in the area was

approximately 5 millirem per hour. Unit 2 began a plant evolution (RCS forced oxygenation) that had the potential to raise radiation levels in several areas of the unit.

Due to the forced oxygenation process, PG&E implemented their posting guides and

restricted personnel access to high radiation areas in Unit 2 that had potentially higher-

-28-than-normal radiation levels. However, PG&E did not restrict personnel access to radiation areas or survey a hallway on the 100-foot elevation that had the potential for higher-than-normal radiation levels prior to allowing personnel to enter them. PG&E's

posting guides did not address any actions that needed to be implemented for radiation

areas or the hallways of the 100-foot elevation. The inspectors determined that PG&E

failed to survey the area to determine the magnitude and extent of the radiation levels

and to evaluate the radiological hazards prior to allowing personnel to enter the area and

whether the posting guides communicated any required action.

Analysis:

The failure to survey is a performance deficiency. The finding was greater than minor because it was associated with the Occupational Radiation Safety

Cornerstone attribute of Exposure Control and Monitoring and affected the cornerstone

objective to ensure the adequate protection of a worker's health and safety from

exposure to radiation because workers could have unknowingly received additional

radiation exposure from the increase in radiation levels. Because the finding involved

the potential for unplanned, unintended dose resulting from conditions that were contrary

to NRC regulations, the finding was evaluated using the Occupational Radiation Safety

Significance Determination Process. The finding was determined to be of very low

safety significance because:

(1) it did not involve as low as reasonably

achievable (ALARA) planning or work controls,

(2) there was no personnel

overexposure,

(3) there was no substantial potential for personnel overexposure, and
(4) the finding did not compromise PG&E's ability to assess dose. The finding had

crosscutting aspects associated with human performance because adequate resources

were not established for the survey requirements.

Enforcement

10 CFR 20.1501(a) requires that each licensee make or cause to be made surveys that may be necessary to comply with the regulations in Part 20 to

determine the extent and magnitude of radiation levels and to evaluate the radiological

hazards. Pursuant to 10 CFR 20.1003, survey means an evaluation of the radiological

conditions and potential hazards incident to the production, use, transfer, release, disposal, or presence of radioactive material or other sources of radiation. Contrary to

this requirement, on April 18, 2006, PG&E failed to survey the 100-foot elevation of the

Unit 2 auxiliary building to assure compliance with 10 CFR 20.1201, which limits

radiation exposure to occupational workers to 5.0 rem total effective dose equivalent.

This violation was entered into PG&E's CAP as AR 0665039. Because this finding is of

very low safety significance and was entered into PG&E's CAP, it is being treated as an

NCV, consistent with Section VI.A.1 of the NRC Enforcement Policy:

NCV 50-323/06-03-04, Failure to Survey to Identify the Magnitude and Extent of

Radiation Levels to Identify Radiological Hazards.2OS2ALARA Planning and Controls (71121.02)

a. Inspection Scope

The inspectors assessed PG&E's performance with respect to maintaining individual and collective radiation exposures ALARA. The inspectors used the requirements in 10 CFR

Part 20 and PG&E's procedures required by TS as criteria for determining compliance.

The inspectors interviewed PG&E personnel and reviewed:

-29-*Five (to 10) outage or on-line maintenance work activities scheduled during the inspection period and associated work activity exposure estimates which were

likely to result in the highest personnel collective exposures *ALARA work activity evaluations, exposure estimates, and exposure mitigation requirements *Integration of ALARA requirements into work procedure and radiation work permit documents *Person-hour estimates provided by maintenance planning and other groups to the radiation protection group with the actual work activity time requirements *Dose rate reduction activities in work planning

  • Workers use of the low dose waiting areas
  • First-line job supervisors' contribution to ensuring work activities are conducted in a dose efficient manner*Radiation worker and radiation protection technician performance during work activities in radiation areas, airborne radioactivity areas, or high radiation areas *Self-assessments, audits, and special reports related to the ALARA program since the last inspection The inspectors completed nine samples.

b. Findings

No findings of significance were identified.4.

OTHER ACTIVITIES

4OA1 PI Verification

.1 Cornerstone:

Occupational Radiation Safety*Occupational Exposure Control Effectiveness

a. Inspection Scope

The inspectors reviewed PG&E's documents from January 1 through March 31, 2006.

The review included corrective action documentation that identified occurrences in

locked high radiation areas (as defined in PG&E's TS), very high radiation areas (as

defined in 10 CFR 20.003), and unplanned personnel exposures (as defined in

NEI 99-02). Additional records reviewed included ALARA records and whole body

counts of selected individual exposures. The inspectors interviewed PG&E personnel

who were accountable for collecting and evaluating the PI data. In addition, the

-30-inspectors toured plant areas to verify that high radiation, locked high radiation, and very high radiation areas were properly controlled. PI definitions and guidance contained in

NEI 99-02, "Regulatory Assessment Indicator Guideline," Revision 3, were used to verify

the basis in reporting for each data element.

The inspectors completed one sample in this cornerstone.

b. Findings

No findings of significance were identified.

.2 Cornerstone:

Public Radiation Safety*Radiological Effluent Technical Specification/Offsite Dose Calculation Manual Radiological Effluent Occurrences

a. Inspection Scope

The inspectors reviewed PG&E's documents from January 1 through March 31, 2006.

PG&E's records reviewed included corrective action documentation that identified

occurrences for liquid or gaseous effluent releases that exceeded PI thresholds and

those reported to the NRC. The inspectors interviewed PG&E personnel who were

accountable for collecting and evaluating the PI data. PI definitions and guidance

contained in NEI 99-02, "Regulatory Assessment Indicator Guideline," Revision 3, were

used to verify the basis in reporting for each data element.

The inspectors completed one sample in this cornerstone.

b. Findings

No findings of significance were identified.4OA2Identification and Resolution of Problems (71152)

.1 Routine Review of Identification and Resolution of Problems

a. Inspection Scope

The inspectors performed a daily screening of items entered into PG&E's CAP. This assessment was accomplished by reviewing ARs and event trend reports and attending

daily operational meetings. The inspectors:

(1) verified that equipment, human

performance, and program issues were being identified by PG&E at an appropriate

threshold and that the issues were entered into the CAP;

(2) verified that corrective

actions were commensurate with the significance of the issue; and

(3) identified

conditions that might warrant additional follow-up through other baseline inspection

procedures.

-31-

b. Findings

No findings of significance were identified.

.2 Selected Issue Follow-Up Inspection

a. Inspection Scope

In addition to the routine review, the inspectors selected the one below listed issue for a more in-depth review. The inspectors considered the following during the review of

PG&E's actions:

(1) complete and accurate identification of the problem in a timely

manner;

(2) evaluation and disposition of operability/reportability issues;
(3) consideration of extent of condition, generic implications, common cause, and

previous occurrences;

(4) classification and prioritization of the resolution of the problem;
(5) identification of root and contributing causes of the problem;
(6) identification of

corrective actions; and

(7) completion of corrective actions in a timely manner.*April 26, 2006: High Stator Temperature Trends on Component Cooling Water Motors Documents reviewed by the inspectors are listed in the attachment.

b. Findings

No findings of significance were identified.

.3 Semiannual Trend Review

a. Inspection Scope

The inspectors completed a semiannual trend review of repetitive or closely-related issues that were documented in ARs, system and component health reports, quality

assurance audits, trend reports, Diablo Canyon internal PIs, and NRC inspection reports

to identify trends that might indicate the existence of more safety-significant issues. The

inspectors' review consisted of the 6-month period of January 1 to June 30, 2006. When

warranted, some of the samples expanded beyond those dates to fully assess the issue.

The inspectors also reviewed CAP items associated with troubleshooting. The

inspectors compared and contrasted their results with the results contained in PG&E's

quarterly trend reports. Corrective actions associated with a sample of the issues

identified in PG&E's trend report were reviewed for adequacy. Documents reviewed by

the inspectors are listed in the attachment.

b. Findings

The inspectors reviewed Quality Verification Assessment 060480001, "Troubleshooting,"

dated April 14, 2006. The purpose of the assessment was to evaluate the

implementation of the troubleshooting program as described in Procedure MA1.DC10, "Troubleshooting," Revision 9. Quality Verification identified a need for improvement in

documentation of problem statements, data acquisition results, determination of possible

-32-failure modes, troubleshooting plans, and analysis of results. In particular, maintenance personnel's implementation of the troubleshooting procedure often did not meet the

troubleshooting attributes, while engineering personnel's implementation of

troubleshooting had only minor inconsistencies. Furthermore, the assessment observed

the need for improvement in the knowledge of troubleshooting requirements throughout

the organization for:

(1) when troubleshooting should be implemented,
(2) what types of

equipment problems require troubleshooting, and

(3) the level of planning and

documentation required for low level equipment problems. Quality verification found that

Procedure MA1.DC10 continued to be difficult to use despite revisions to the procedure.

The inspectors also reviewed previous Quality Verification assessments, dating back to 2004, for troubleshooting observations. These assessments are listed in the

attachment. While the assessments pointed out that the site has shown improvement in troubleshooting efforts since 2003, the inspectors observed that Quality Verification had

previously identified similar issues as those discussed above. The following are some

insights from previous assessments, which also covered previous revisions to

Procedure MA1.DC10.*In some instances, initial troubleshooting efforts failed to identify the cause of the problem for safety-related and/or risk-significant equipment.*On several occasions, the site was reluctant to enter a more rigorous/formal troubleshooting format, since it was seen as time consuming and the technicians

felt they knew better on how to approach the problem as opposed to following

Procedure MA1.DC10. As a result, there were instances where the cause

determination was inaccurate, such as the case with Containment Spray

Pump 2-2 control cable ground.*Procedure MA1.DC10 was deficient, making it difficult for maintenance personnel to comply with its requirements. Subsequently, personnel performing

troubleshooting relied upon their knowledge and experience to the exclusion of

the requirements in the troubleshooting procedure.*In some instances, maintenance and engineering personnel were reluctant to characterize work activities as "troubleshooting" when in fact the activities

involved the investigation of plant equipment problems. Quality Verification

recommended that senior management emphasize the expectations for

implementing Procedure MA1.DC10 when the criteria for entering the procedure

were met.*Quality Verification noted that the level of detail in troubleshooting documentation was weak. For example, as-found conditions were not documented, results of a

component history search were not documented, and documentation of work

performed was not detailed.

The inspectors have observed several troubleshooting activities that have occurred on site and, in general, agree with the assessments identified by Quality Verification. Most

recently, the inspectors observed troubleshooting for AFW Discharge

Valves FW-1-LCV-107 and FW-1-LCV-108, as described in Section

4OA5 of this report.

-33-The inspectors observed that troubleshooting for Valve FW-1-LCV-107 was performed by maintenance personnel. In reviewing the documentation from that troubleshooting

effort, the inspectors could not identify any other possible failure mechanisms that had

been considered by Maintenance personnel other than the determined cause.

Additionally, the inspectors observed data that would tend to contradict the determined

cause of the valve, as described in Section 4OA5. The inspectors also observed

troubleshooting for Valve FW-1-LCV-108, which had similar indications as Valve

FW-1-LCV-107 when it failed to stroke. The troubleshooting team consisted of both

Engineering and Maintenance personnel. The inspectors observed that the Engineering

personnel were careful to:

(1) preserve evidence by arranging the various investigative

activities,

(2) consider various potential failu re mechanisms before investigative activities began, and
(3) consider all data available to them. In summary, the inspectors felt that

the observations made during the troubleshooting on Valves FW-1-LCV-107

and FW-1-LCV-108 confirmed the observations documented by Quality Verification in their assessments.

.4 Occupational Radiation Safety

a. Inspection Scope

The inspectors evaluated the effectiveness of PG&E's problem identification and resolution process with respect to the following inspection areas:*Access Control to Radiologically Significant Areas (Section 2OS1)*ALARA Planning and Controls (Section 2OS2)

b. Findings

No findings of significance were identified.

.5 Inservice Inspection

a. Inspection Scope

The inspector reviewed the related condition reports on an inservice inspection issued during the current and past refueling outages and verified that PG&E identified, evaluated, corrected, and trended problems. The inspector evaluated the effectiveness

of PG&E's CAP, including the adequacy of the technical resolutions.

b. Findings

No findings of significance were identified.

-34-4OA3Event Followup (71153)

.1 Main Turbine Trip Due to Personnel Error

a. Inspection Scope

On June 7, 2006, the inspector reviewed the actions taken prior to, during, and following a main turbine trip on Unit 2, on May 25, 2006. Operations personnel were attempting to

parallel the main generator to the grid during the reactor startup, following a refueling

outage.

b. Findings

No findings of significance were identified.

.2 (Closed) Licensee Event Report 50-275/1-2005-001-00 Steam Generator Tube Plugging

Because of Stress Corrosion Cracking On November 11, 2005, PG&E determined that analysis of eddy current testing on Steam Generators 1-1 and 1-2 indicated that greater than one percent of the tubes were

defective as a result of outside diameter stress corrosion cracking at the hot leg tube

support plates and at the hot leg top of tubesheet. This determination occurred at the

end of Operating Cycle 13. The inspector verified that PG&E took effective corrective

action. All defective tubes were plugged and removed from service in accordance with

TS 5.5.9, "Steam Generator (SG) Tube Surveillance Program." The licensing basis accident analysis assumes a tube plugging limit of 15 percent per steam generator. The

plugging percentage for each Unit 1 steam generator remains within the current

allowable limit of 15 percent. Steam Generator 1-1 has 6.8 percent plugged and Steam

Generator 1-2 has 9.3 percent plugged. PG&E maintains a comprehensive program to

minimize steam generator tube degradation and plans to replace the steam generators

at the end of Operating Cycle 15. This licensee event report is closed.

4OA5Other

.1 TI 2515/160 - Pressurizer Penetration Nozzles and Steam Space Piping Connections in

U.S. Pressurized Water Reactors

a. Inspection Scope

The inspectors reviewed PG&E's actions regarding the inspection and repair associated with Alloy 82/182/600 material that may have been used in pressurizer penetration

nozzles, steam space piping connections, heads, and shells. Specifically, the inspectors

reviewed PG&E's response to NRC Bulletin 2004-01, "Inspection of Alloy 82/182/600

Materials Used in the Fabrication of Pressurizer Penetrations and Steam Space Piping

Connections at Pressurized Water Reactors." PG&E documented in their response to

the bulletin that the Unit 2 pressurizer utilized Alloy 82/182 material in the nozzle to safe

end welds for the surge line, the pressurizer safety lines, the power-operated relief valve

-35-lines, and the spray line. Stainless steel was used in all other pressurizer penetration welds. In PG&E's response to the bulletin, they committed to a bare metal visual exam

of all the welds that had Alloy 82/182 material.

The inspectors reviewed PG&E's response to NRC Bulletin 2004-01 and observed their inspection activities for the Unit 2 pressurizer. The inspectors verified the qualifications

of personnel performing the bare metal exam and independently observed several of the

subject pressurizer penetration welds for evidence of boric acid deposits and the

capability to perform the bare metal exam. The inspectors reviewed Procedure ISI VT 2-1, "Visual Examination During Section XI System Pressure Test,"

Revision 0, during the inspection.

The activities required in Temporary Instruction (TI) 2515/160 for Diablo Canyon Power Plant Unit 2 have been completed. Documents reviewed by the inspectors are listed in

the attachment. This TI is closed for Unit 2.

b. Findings

No findings of significance were identified.

.2 TI 2515/165 - Operational Readiness of Offsite Power and Impact on Plant Risk

a. Inspection Scope

The objective of TI 2515/165, "Operational Readiness of Offsite Power and Impact on Plant Risk," is to gather information to support the assessment of nuclear power plant

operational readiness of offsite power systems and impact on plant risk. During this

inspection, the inspectors interviewed PG&E personnel, reviewed applicable procedures, and gathered information for further evaluation by the Office of Nuclear Reactor

Regulation.

b. Findings

No findings of significance were identified.

.3 (Closed) Unresolved Item (URI) 05000275/05-05-03:

Corrective Actions to Prevent Repetitive Failures of AFW Limitorque Valves

a. Inspection Scope

The inspectors performed additional inspection associated with this URI to determine any performance issues associated with design and maintenance practices regarding

Limitorque actuators. The inspectors also evaluated any extent of condition and/or

generic impacts.

b. Findings

Introduction

A Green, NRC-identified NCV was identified for the failure to correct a significant condition adverse to quality as required by 10 CFR Part 50, Appendix B,

-36-Criterion XVI, "Corrective Action." Specifically, PG&E failed to preclude repetition of similar failures with Limitorque Model SMB-000 motor-operated valves in the AFW

system. The failure of these motor-operated valves affected the ability of the valves to

be operated from the control room and the hot shutdown panel. These valves are

required to shut in the event of a faulted steam generator or to prevent overfilling of a steam generator.

Description

The AFW system is an engineered safety feature system that is directly relied upon to prevent core damage and RCS overpressurization in the event of

transients, such as a loss of normal feedwater or secondary system pipe rupture. It also

provides a means for plant cooldown following any plant transient.

Motor-operated Valves FW-1-LCV-107, FW-1-LCV-108, and FW-1-LCV-109 are discharge isolation valves associated with the turbine-driven AFW pump. On

March 15, 2003, Valve FW-2-LCV-109 failed to close during routine surveillance testing.

Operators failed to preserve the faulted condition by remotely opening the valve, manually stroking the valve, removing the actuator cover and inspecting the contacts, and burnishing the close torque contacts. Because the failure was not repeated during

troubleshooting, PG&E staff determined that it was not a maintenance preventable

functional failure. However, PG&E staff identified in AR A0578562 that this was a critical

component failure that should be prevented from recurring per Procedure ER1.ID1, "Equipment Reliability Process," Revision 1.

On August 20, 2004, Valve FW-1-LCV-107 failed to operate after corrective maintenance. PG&E staff identified in AR A0616766 that this failure was a maintenance

preventible functional failure and directed staff to implement actions to prevent

recurrence. The corrective action identified was to revise Procedure MP E-53.10A, "Preventive Maintenance of Limitorque Operators," to include steps to burnish the torque

switch contacts, since the cause of the valve to stroke was determined to be corrosion.

On November 3, 2005, operators were performing a functional test of Valve FW-1-LCV-107 per Procedure STP V-2U2D, "Exercising S/G No. 2 AFW Supply

Valves LCV-107 and LCV-108," Revision 4, after valve packing had been replaced.

Motor-operated Valve FW-1-LCV-107 had been stroked open and closed successfully

from the control room. Operational control for the valve was then transferred to the Hot

Shutdown Panel, the valve was opened and not able to be shut. A second attempt to

shut the valve was unsuccessful. Records of the subsequent visual inspection indicated

that the contact fingers were coated with debris, but not the contact surfaces.

Maintenance records also indicated that the actuator cover was removed and the torque

switch contacts were burnished. The valve was declared operable after several

successful operations. PG&E staff identified this problem in AR A0650104 and again

directed that this problem be prevented from recurring.

On February 2, 2006, a similar failure occurred with Valve FW-1-LCV-108. This valve also had successful operations following maintenance with a subsequent failure.

Troubleshooting by PG&E staff determined that the torque limit switch contacts had high

resistance. During troubleshooting efforts, the inspectors observed that the contact

switch housing cover for the Limitorque Model SMB-000 actuators had been modified to

allow them to fit over the contact assembly more easily. The inspectors also observed

-37-that, even with the modified cover, the installation and removal of the close-fitting cover rubbed against the wires. PG&E troubleshooting personnel determined that the screws

would loosen if the wires leading to the torque switch were moved.

The inspectors verified that the installation of the cover and potential for screw loosening by wire movement could contribute to valves failing to actuate, which had not been

previously evaluated by PG&E staff as a possible contributor to the failures of

Valve FW-1-LCV-107. PG&E initiated a root cause evaluation into the failure of the

Model SMB-000 actuators (Nonconformance Report NCR N0002205) and identified

organizational deficiencies in the failure analysis of critical components as the root

cause. The root cause determined that PG&E staff failed to account for maintenance

practices, latent design issues, or environmental effects other than corrosion to prevent

repeat failures of Model SMB-000 actuators.

The inspectors determined that PG&E staff failed to promptly identify and correct a significant condition adverse to quality. Specifically, the inspectors determined that

PG&E failed to adequately troubleshoot the failures of Valve FW-1-LCV-107. During the

inspection, data such as:

(1) the failure of the valves to stroke after one or more

successful strokes,

(2) the conductance capability of the silver torque switch contacts

with corrosion,

(3) the orientation of the torque switch contacts, and
(4) an already

present step in the maintenance procedure to clean the torque switch contacts lead the

inspectors to question the troubleshooting conclusion of debris or corrosion on the

torque switch contacts. Furthermore, the troubleshooting results from

Valve FW-1-LCV-108 reduced the likelihood of debris or corrosion as a possible failure

mechanism. The inspectors determined that, with the history of similar failures of these

type of valve actuators, along with the si gnificance of the system, PG&E should have initiated a root cause evaluation earlier with the Valve FW-1-LCV-107 failures to prevent

recurrence of the problem.

Analysis:

The performance deficiency associated with this finding was the failure to promptly identify and correct a significant condition adverse to quality associated with

the AFW motor-operated discharge valves. The finding is greater than minor because it

is associated with the Mitigating Systems Cornerstone attribute of equipment

performance and affects the associated cornerstone objective to ensure the availability, reliability, and capability of systems that respond to initiating events to prevent

undesirable consequences. Using the IMC 0609, "Significance Determination Process,"

Phase 1 Worksheet, the finding is determined to be of very low safety significance

because it did not represent an actual loss of safety function, represent an actual loss of

safety function for a single train for greater than the TS allowed outage time, or screen

as potentially risk significant due to seismic, fire, flooding, or severe weather initiating

events. The finding had a crosscutting aspect in the area of problem identification and

resolution since PG&E staff failed to adequately trend, assess, and troubleshoot

previous Limitorque SMB-000 actuator failures.

Enforcement:

10 CFR Part 50, Appendix B, Criterion XVI, states, in part, that measures shall be established to assure that conditions adverse to quality, such as failures, malfunctions, deficiencies, deviations, defective material and equipment, and

nonconformances, are promptly identified and corrected. In the case of significant

conditions adverse to quality, the measures shall assure that the cause of the condition

-38-is determined and corrective action taken to preclude repetition. Contrary to this, from 2003 to 2006, PG&E staff failed to identify and implement adequate corrective actions to

prevent recurrence of turbine-driven AFW Limitorque SMB-000 actuator failures. Since

failure to identify and prevent recurrence of a significant condition adverse to quality was

determined to be of very low safety significance and has been entered into the CAP as

Nonconformance Report N0002205, this violation is being treated as a NCV, consistent

with Section VI.A of the NRC Enforcement Policy: NCV 50-275/06-03-05, Failure to

Prevent Recurrence of Limitorque Model SMB-000 Failures.40A6Management Meetings

Exit Meeting Summary

On April 6, 2006, the inspectors discussed the inspection results of licensed operator requalification with Mr. David Burns, Operations Training Supervisor. PG&E

acknowledged the findings presented. The inspectors asked PG&E if any materials

examined during the inspection should be considered proprietary. No proprietary

information was identified.

On April 10, 2006, the inspectors conducted a telephonic exit meeting to present the inspection results on Emergency Action Level and Emergency Plan Changes to

Mr. R. Waltos, Supervisor, Emergency Planning, who acknowledged the findings. The

inspectors confirmed that proprietary info rmation was not provided or examined during the inspection.

The inspector presented the results of the inservice inspection effort to Mr. J. Becker, Vice President Diablo Canyon Operations and Station Director, and other members of

PG&E management on May 3, 2006. PG&E management acknowledged the inspection

findings. During the inspection, the inspector asked if any materials examined should be

considered proprietary. Several documents were identified as proprietary information by

PG&E. The inspector informed PG&E that copies of those documents would be

destroyed after their review.

On May 4, 2006, the inspectors presented the occupational radiation safety inspection results to Mr. J. Becker, Vice President Diablo Canyon Operations and Station Director, and other members of the staff who acknowledged the findings. The inspectors

confirmed that proprietary information was not provided or examined during the inspection.

The resident inspection results were presented on July 12, 2006, to Mr. J. Becker, Vice President Diablo Canyon Operations and Station Director, and other members of PG&E

management. PG&E acknowledged the findings presented. The inspectors asked

PG&E whether any materials examined during the inspection should be considered

proprietary. No proprietary information was reviewed by the inspectors.

ATTACHMENT:

SUPPLEMENTAL INFORMATION

KEY POINTS OF CONTACT

PG&E personnel

J. Becker, Vice President - Diablo Canyon Operations and Station Director
S. David, Manager, Operations
J. Fledderman, Director, Site Services
R. Hite, Manager, Radiation Protection
D. Jacobs, Vice President - Nuclear Services
S. Ketelsen, Acting Director, Nuclear Quality, Analysis, and Licensing
K. Peters, Director, Engineering Services
J. Purkis, Director, Maintenance Services
P. Roller, Director, Operations Services
D. Taggart, Manager, Quality Verification
R. Waltos, Supervisor, Emergency Planning

LIST OF ITEMS OPENED, CLOSED, AND DISCUSSED

Opened

None

Opened and Closed50-323/06-03-01NCVFailure to Follow Welding Procedures (Section 1R08)50-275/06-03-02NCVFailure to Promptly Identify Voiding in Accumulator

Discharge Line (Section 1R15)50-323/06-03-03NCVInadequate Refueling Procedure for Draining and

Depressurizing the Reactor Coolant System

(Section 1R20)50-323/06-03-04NCVFailure to Survey to Identify the Magnitude and Extent of

Radiation Levels to Identify Radiological Hazards

(Section 2OS1)50-275/06-03-05NCVFailure to Prevent Recurrence of Limitorque Model

SMB-000 Failures (Section 4OA5.3)

Closed

05000275/2005-05-03URICorrective Actions to Prevent Repetitive Failures of

Auxiliary Feedwater Limitorque Valves

A-250-275/1-2005-001-00LERSteam Generator Tube Plugging Because of Stress

Corrosion Cracking (Section 4OA3.1)

LIST OF DOCUMENTS REVIEWED