IR 05000461/2006010: Difference between revisions

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| issue date = 12/21/2006
| issue date = 12/21/2006
| title = IR 05000461-06-010 (DRS) on 11/13/2006 Through 11/30/2006 for Clinton Power Station. Routine Engineering Baseline Inspection
| title = IR 05000461-06-010 (DRS) on 11/13/2006 Through 11/30/2006 for Clinton Power Station. Routine Engineering Baseline Inspection
| author name = Hills D E
| author name = Hills D
| author affiliation = NRC/RGN-III/DRS/EB1
| author affiliation = NRC/RGN-III/DRS/EB1
| addressee name = Crane C M
| addressee name = Crane C
| addressee affiliation = Exelon Generation Co, LLC, Exelon Nuclear
| addressee affiliation = Exelon Generation Co, LLC, Exelon Nuclear
| docket = 05000461
| docket = 05000461
Line 18: Line 18:


=Text=
=Text=
{{#Wiki_filter:
{{#Wiki_filter:December 21, 2006Mr. Christopher M. CranePresident and Chief Nuclear Officer Exelon Nuclear Exelon Generation Company, LLC 4300 Winfield Road Warrenville, IL 60555SUBJECT:CLINTON POWER STATION NRC EVALUATION OF CHANGES, TESTS, OR EXPERIMENTS AND PERMANENT PLANT MODIFICATIONS BASELINE INSPECTION REPORT 05000461/2006010(DRS)
[[Issue date::December 21, 2006]]
 
Mr. Christopher M. CranePresident and Chief Nuclear Officer Exelon Nuclear Exelon Generation Company, LLC 4300 Winfield Road Warrenville, IL 60555
 
SUBJECT: CLINTON POWER STATION NRC EVALUATION OF CHANGES, TESTS, OR EXPERIMENTS AND PERMANENT PLANT MODIFICATIONS BASELINE INSPECTION REPORT 05000461/2006010(DRS)


==Dear Mr. Crane:==
==Dear Mr. Crane:==
On November 30, 2006, the U.S. Nuclear Regulatory Commission (NRC) completed acombined baseline inspection of the Evaluation of Changes, Tests, or Experiments and Permanent Plant Modifications at the Clinton Power Station. The enclosed report documents the results of the inspection, which were discussed with Mr. B. Hanson, and others of your staffat the completion of the inspection on November 30, 2006.The inspectors examined activities conducted under your license as they relate to safety andcompliance with the Commission's rules and regulations, and with the conditions of your license. The inspectors reviewed selected procedures and records, observed activities, and interviewed personnel. Based on the results of the inspection, no findings of significance were identified.In accordance with 10 CFR Part 2.390 of the NRC's "Rules of Practice," a copy of this letterand its enclosure will be available electronically for public inspection in the NRC PublicDocument Room, or from the Publicly Available Records (PARS) component of NRC's C. Crane-2-document system (ADAMS), accessible from the NRC Web site at http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room).
On November 30, 2006, the U.S. Nuclear Regulatory Commission (NRC) completed acombined baseline inspection of the Evaluation of Changes, Tests, or Experiments and Permanent Plant Modifications at the Clinton Power Station. The enclosed report documents the results of the inspection, which were discussed with Mr. B. Hanson, and others of your staffat the completion of the inspection on November 30, 2006.The inspectors examined activities conducted under your license as they relate to safety andcompliance with the Commission's rules and regulations, and with the conditions of your license. The inspectors reviewed selected procedures and records, observed activities, and interviewed personnel. Based on the results of the inspection, no findings of significance were identified.In accordance with 10 CFR Part 2.390 of the NRC's "Rules of Practice," a copy of this letterand its enclosure will be available electronically for public inspection in the NRC PublicDocument Room, or from the Publicly Available Records (PARS) component of NRC's C. Crane-2-document system (ADAMS), accessible from the NRC Web site at http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room).


Sincerely,/RA/David E. Hills, ChiefEngineering Branch 1 Division of Reactor SafetyDocket No. 50-461License No. NPF-62
Sincerely,
 
/RA/David E. Hills, ChiefEngineering Branch 1 Division of Reactor SafetyDocket No. 50-461License No. NPF-62Enclosure:Inspection Report 05000461/2006010(DRS) w/attachment: Supplemental Informationcc w/encl:Site Vice President - Clinton Power StationPlant Manager - Clinton Power Station Regulatory Assurance Manager - Clinton Power Station Chief Operating Officer Senior Vice President - Nuclear Services Vice President - Operations Support Vice President - Licensing and Regulatory Affairs Manager Licensing - Clinton Power Station Senior Counsel, Nuclear, Mid-West Regional Operating Group Document Control Desk - Licensing Assistant Attorney General Illinois Emergency Management Agency State Liaison Officer, State of Illinois Chairman, Illinois Commerce Commission
===Enclosure:===
Inspection Report 05000461/2006010(DRS)  
 
===w/attachment:===
Supplemental Informationcc w/encl:Site Vice President - Clinton Power StationPlant Manager - Clinton Power Station Regulatory Assurance Manager - Clinton Power Station Chief Operating Officer Senior Vice President - Nuclear Services Vice President - Operations Support Vice President - Licensing and Regulatory Affairs Manager Licensing - Clinton Power Station Senior Counsel, Nuclear, Mid-West Regional Operating Group Document Control Desk - Licensing Assistant Attorney General Illinois Emergency Management Agency State Liaison Officer, State of Illinois Chairman, Illinois Commerce Commission


=SUMMARY OF FINDINGS=
=SUMMARY OF FINDINGS=
Line 107: Line 97:
The following is a list of licensee documents reviewed during the inspection, includingdocuments prepared by others for the licensee.
The following is a list of licensee documents reviewed during the inspection, includingdocuments prepared by others for the licensee.
: Inclusion on this list does not imply that NRC
: Inclusion on this list does not imply that NRC
inspectors reviewed the documents in their entirety, but rather, that selected sections or portions of the documents were evaluated as part of the overall inspection effort.
: Inclusion of a document in this list does not imply NRC acceptance of the document, unless specifically statedin the inspection report.IR02Evaluation of Changes, Tests, or Experiments (71111.02)10
: CFR 50.59 ScreeningsCL-2004-S-001; V-TIP Change to Add Allowance for Battery Equalizing at 2.5 VPC;dated January 7, 2004CL-2004-S-007; Diesel Generator Diagnostic Testing; dated January 30, 2004
: CL-2004-S-010; 24-Month - Revise Division I, II, and III 4.16 kV Buses UndervoltageRelays (Degraded Voltage Relays) Operate and Reset Voltage Set-points; dated February 4, 2004CL-2004-S-021; Add SX Division I, II, and III Vacuum Breakers to Mitigate WaterHammer; dated February 26, 2004CL-2004-S-029; Revise Setpoint for Ground Detection Relay 1X1R-DC090 in DC MCC1F (1DC17E); dated March 18, 2004CL-2004-S-035; 1SX303A/B; Active Safety Function; dated April 24, 2004
: CL-2004-S-074; Redesign of Check Valve 1N66F130 and Installation of an IsolationValve on Line 1OG92A-1; dated October 1, 2004CL-2004-S-084; Changes to Bases Sections B3.3.4.1 and B3.3.6.1; datedNovember 18, 2004CL-2005-S-002; Change the Sudden Pressure Relay Trip Logic for the Unit AuxiliaryTransformers (1AP01EA and 1AP01EB) from a One-Out-Of-One (1/1) Scheme to a Two-Out-Of-Two (2/2) Scheme; dated March 10, 2005CL-2005-S-008; ORM 2.4.9, Essential Switchgear Room (VX) Ventilation; datedMay 25, 2005CL-2005-S-009; Revise Delay Period for Missed Testing Requirements, Section 1.3.3;dated March 29, 2005CL-2005-S-018r1; Reroute RCIC Head Spray Piping to Avoid Hydrogen Accumulation;dated November 7, 2005
: 3CL-2005-S-046; Swing Battery Charger (1DC11E) to Supply 125 Vdc Power toDivision 1 MCC 1A (1DC13E) While Division I Battery Charger (1DC06E) is Removed from Service for Preventive Maintenance; dated July 25, 2005CL-2005-S-052; 24-Month Refuel Cycle Project - ORM 4.5.2.1a MOV Thermal OverloadProtection - Frequency Change; August 15, 2005CL-2005-S-060; USAR Change No. 2005-028; dated September 22, 2005
: CL-2005-S-069; Bypass High Water Temperature Switch S11 for the Division III; datedNovember 21,
: 200510
: CFR 50.59 EvaluationsCL-2004-E-078; RPV Core Shroud Repair; dated March 11, 2005
: CL-2005-E-041; To Provide a Temporary Vent Path for the RHR Shutdown CoolingSuction Header; dated June 27, 2005CL-2006-E-002; Interim Abandonment of RT Pump "C"; dated January 17, 2006
: CL-2006-E-003; Increase ORM Acceptance Criteria for EFCVs 1CM066 and 1CM067;dated February 23, 2006IR17Permanent Plant Modifications (71111.17B)ModificationsEC
: 348071; LPCS/RHR-A Internal Line Break Setpoint Revision for Transmitter1E31N080A; Revision 0EC
: 359047; Issue Design for Alternate Motor for 0VC03CA Fan; Revision 0
: EC 351756; PLU K1 Relay has a Scram Potential; Revision 0
: EC 353793; Replace Obsolete BOP 1E DC Main Feed Breaker with Fused DisconnectAssembly; Revision 0EC
: 357284; CO2/Diesel Generator Ventilation (VD) Relay Replacement EC Requiredfor Closure of OP Evaluation
: IR 300035; Revision 0EC
: 358913; Formalize Voltage Profile for MOV 1E22-F012; Revision 0
: EC 359047; Issue Design for Alternate Motor for 0VC03CA Fan; Revision 0
: Commercial Grade DedicationsCGD 46343; Diesel Generator Circulating Lube Oil Pump Discharge Check Valve SealKit; dated October 20, 2005
: 4Equivalency EvaluationsIEE 34648; Item Equivalency Evaluation for Using
: CR 120BD05041 Relay as anAlternate to the Existing ITE/Gould J13 Relay; Revision 0IEE 36867; Item Equivalency Evaluation for a Molded Case Circuit Breaker HandleMaterial Change; Revision 0IEE 50980; Item Equivalency Evaluation for a Molded Case Circuit BreakerQualification; Revision 0 Other Documents Reviewed During InspectionCorrective Action Program Documents Generated As a Result of InspectionIR00558772; 50.59 Inspection Identified Reference Error in
: CL-2004-S-029; datedNovember 16, 2006IR00558788; USAR Chapter 3 References IWP Code That Is No Longer Used; datedNovember 16, 2006IR00560840; 50.59 and USAR Inconsistency; dated November 21, 2006
: Corrective Action Program Documents Reviewed During the Inspection
: IR295012; Excessive Oil Leakage Observed for MPT "A"; dated January 27, 2005
: IR342801 and Op Eval
: 342801-02; RHR Shutdown Cooling Suction Isolation ValvesLeaking Past Their Seats; Revision 1IR359292; Key Modification Objective Not Achieved; dated August 3, 2005
: IR488071; Received Annunciator 5011-8F, ERAT SVC TROUBLE; dated May 8, 2006
: IR448363; Excess Flow Check Valve 1CM066 Closed at 1.05 gpm; datedFebruary 1, 2006IR449951; EC347160 Not Routed for Ops DAR Yet Procedures are Impacted; datedDecember 12, 2006IR494152; WO Pump Motor Breaker Settings Lower than Standard Practice; datedMay 26, 2005IR495509; Alarm Response Procedures Not Revised to Reflect Engineering Change;June 1, 2006IR508667; 50.59 Screen Not Revised for Revision 3 of EC; dated July 17,2006
: IR 516896; Emergency Diesel Generator USAR Discrepancy; dated August 4, 2006
: 5CalculationsAnalysis No. 19-AN-19; Calculations for Functional Requirements for 1
st and 2 nd LevelUndervoltage Relays at 4 kV Buses 1A1, 1B1, and 1C1; Revision 3Analysis No. 19-AK-13; Analysis of Load Flow, Short Circuit and Motor Starting UsingETAP Power Station; Revision 0Analysis No. 19-D-08; 125V DC MCC 1E and 1F Circuit Breaker Settings; Revision 2D
: Analysis No. 19-D-12; Setting for 125 VDC Ground Detecting Voltmeters; Revision 0
: DrawingsE02-1AP03; Electrical Loading Diagram; Revision Z
: E02-1DC04; Key Diagram 125V DC MCC 1E (1DC16E); Revision 9
: AE-CLT6-1DC09; DC MCC 1E 1DC16E Ground Fault; Revision 0
: AE-CLT6-1DC090; DC MCC 1E 1DC17E Ground Fault; Revision 0
: ProceduresCPS 3310.01; Reactor Core Isolation Cooling (RI); Revision 26
: CPS 3211.01; Shutdown Service Water (SX); Revision 6
: CPS 3303.01; Reactor Water Cleanup (RT); Revision 30
: CPS 5000.01; Alarm Panel 5000 Annunciators - Row 1; Revision 25a
: CPS 9054.02; Reactor Core Isolation Cooling Valve Operability Checks; Revision 36
===Miscellaneous===
: DocumentsFASA AT No.
: 476070; Modifications and 10 CFR50.59 Reviews; dated July 13, 2006
: IST Program Plan; dated October 18, 2006
: Work OrdersWO00751954; MPT 1C Oil Leak; dated February 21, 2005
: WO00756473; MPT 1A Oil leaks; dated November 18, 2004
: WO00906708; RHR Out-of-Service Alarm Due to 1E31-N680A; dated May 19, 2006
: 6
==LIST OF ACRONYMS==
USEDADAMSAgency-Wide Document Access and Management SystemCFRCode of Federal Regulations
DRPDivision of Reactor Projects
DRSDivision of Reactor Safety
ECEngineering Change
IMCInspection Manual Chapter
IRInspection Report
MCCMotor Control Center
NCVNon-Cited Violation
NEINuclear Energy Institute
NRCNuclear Regulatory Commission
ORMOperations Requirements Manual
PARSPublicly Available Records
RHRResidual Heat Removal
SDPSignificance Determination Process
SRSurveillance Requirement
TSTechnical Specifications
: [[USARU]] [[pdated Safety Analysis Report]]
}}
}}

Revision as of 07:32, 13 July 2019

IR 05000461-06-010 (DRS) on 11/13/2006 Through 11/30/2006 for Clinton Power Station. Routine Engineering Baseline Inspection
ML063550210
Person / Time
Site: Clinton Constellation icon.png
Issue date: 12/21/2006
From: Dave Hills
NRC/RGN-III/DRS/EB1
To: Crane C
Exelon Generation Co, Exelon Nuclear
References
IR-06-010
Download: ML063550210 (14)


Text

December 21, 2006Mr. Christopher M. CranePresident and Chief Nuclear Officer Exelon Nuclear Exelon Generation Company, LLC 4300 Winfield Road Warrenville, IL 60555SUBJECT:CLINTON POWER STATION NRC EVALUATION OF CHANGES, TESTS, OR EXPERIMENTS AND PERMANENT PLANT MODIFICATIONS BASELINE INSPECTION REPORT 05000461/2006010(DRS)

Dear Mr. Crane:

On November 30, 2006, the U.S. Nuclear Regulatory Commission (NRC) completed acombined baseline inspection of the Evaluation of Changes, Tests, or Experiments and Permanent Plant Modifications at the Clinton Power Station. The enclosed report documents the results of the inspection, which were discussed with Mr. B. Hanson, and others of your staffat the completion of the inspection on November 30, 2006.The inspectors examined activities conducted under your license as they relate to safety andcompliance with the Commission's rules and regulations, and with the conditions of your license. The inspectors reviewed selected procedures and records, observed activities, and interviewed personnel. Based on the results of the inspection, no findings of significance were identified.In accordance with 10 CFR Part 2.390 of the NRC's "Rules of Practice," a copy of this letterand its enclosure will be available electronically for public inspection in the NRC PublicDocument Room, or from the Publicly Available Records (PARS) component of NRC's C. Crane-2-document system (ADAMS), accessible from the NRC Web site at http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room).

Sincerely,

/RA/David E. Hills, ChiefEngineering Branch 1 Division of Reactor SafetyDocket No. 50-461License No. NPF-62Enclosure:Inspection Report 05000461/2006010(DRS) w/attachment: Supplemental Informationcc w/encl:Site Vice President - Clinton Power StationPlant Manager - Clinton Power Station Regulatory Assurance Manager - Clinton Power Station Chief Operating Officer Senior Vice President - Nuclear Services Vice President - Operations Support Vice President - Licensing and Regulatory Affairs Manager Licensing - Clinton Power Station Senior Counsel, Nuclear, Mid-West Regional Operating Group Document Control Desk - Licensing Assistant Attorney General Illinois Emergency Management Agency State Liaison Officer, State of Illinois Chairman, Illinois Commerce Commission

SUMMARY OF FINDINGS

IR 05000461/2006010(DRS); 11/13/2006 through 11/30/2006; Clinton Power Station. Routineengineering baseline inspection.The inspection covered a 2-week announced baseline inspection on evaluations of changes,tests, or experiments and permanent plant modifications. The inspection was conducted by two regional based engineering inspectors. No violations were identified. The NRC's program for overseeing the safe operation of commercial nuclear power reactors is described in NUREG-1649, "Reactor Oversight Process," Revision 3; dated July 2000.A.Inspector-Identified and Self-Revealed Findings

Cornerstone: Mitigating SystemsNo findings of significance were identified.

B.Licensee-Identified Violations

No findings of significance were identified.

2

REPORT DETAILS

1.REACTOR SAFETYCornerstones: Initiating Events, Mitigating Systems, and Barrier Integrity1R02Evaluations of Changes, Tests, or Experiments (71111.02).1Review of 10 CFR 50.59 Evaluations and Screenings

a. Inspection Scope

From November 13 through November 30, 2006, the inspectors reviewed fourevaluations performed pursuant to 10 CFR 50.59. The inspectors reviewed the evaluations to confirm that they were thorough and that prior NRC approval was obtained as appropriate. The inspector could not review the minimum sample size of five evaluations because the licensee only performed four evaluations during the biennial sample period. The inspectors also reviewed sixteen screenings where licensee personnel had determined that a 10 CFR 50.59 evaluation was not necessary.

In addition, three procedure changes were reviewed to verify they did not meet the applicability requirements for a screening. The evaluations and screenings were chosen based on risk significance, safety significance, and complexity. The list of documents reviewed by the inspectors are included as an attachment to this report.The inspectors used, in part, Nuclear Energy Institute (NEI) 96-07, "Guidelines for 10 CFR 50.59 Implementation," and Revision 1, to determine acceptability of the completed evaluations, and screenings. The NEI document was endorsed by the NRC in Regulatory Guide 1.187, "Guidance for Implementation of 10 CFR 50.59, Changes, Tests, and Experiments," dated November 2000. The inspectors also consulted Part 9900 of the NRC Inspection Manual, "10 CFR Guidance for 10 CFR 50.59, Changes, Tests, and Experiments."

b. Findings

No findings of significance were identified.

1R17 Permanent Plant Modifications (71111.17B).1Review of Permanent Plant Modifications

a. Inspection Scope

From November 13 through November 30, 2006, the inspectors reviewed sevenpermanent plant modifications that had been installed in the plant during the last two years. In addition, the inspectors reviewed three equivalency evaluations and one commercial grade dedication. The modifications were chosen based upon risk significance, safety significance, and complexity. As per inspection procedure 71111.17B, one modification was chosen that affected the barrier integrity cornerstone.

The inspectors reviewed the modifications to verify that the completed design changes 3were in accordance with the specified design requirements, and the licensing bases,and to confirm that the changes did not adversely affect any systems' safety function.

Design and post-modification testing aspects were verified to ensure the functionality of the modification, its associated system, and any support systems. The inspectors also verified that the modifications performed did not place the plant in an increased risk configuration.The inspectors also used applicable industry standards to evaluate acceptability of themodifications. The list of modifications and other documents reviewed by the inspectors is included as an attachment to this report.

b. Findings

No findings of significance were identified.4.OTHER ACTIVITIES (OA)4OA2Identification and Resolution of Problems.1Routine Review of Condition Reports

a. Inspection Scope

From November 13 through November 30, 2006, the inspectors reviewed ten CorrectiveAction Process documents that identified or were related to 10 CFR 50.59 evaluations and permanent plant modifications. The inspectors reviewed these documents to evaluate the effectiveness of corrective actions related to permanent plant modifications and evaluations for changes, tests, or experiments issues. In addition, corrective action documents written on issues identified during the inspection were reviewed to verify adequate problem identification and incorporation of the problems into the corrective action system. The specific corrective action documents that were sampled and reviewed by the inspectors are listed in the attachment to this report.

b. Findings

No findings of significance were identified.

OTHER ACTIVITIES

4OA6Meetings.1Exit MeetingThe inspectors presented the inspection results to Mr. B. Hanson and others of thelicensee's staff, on November 30, 2006. Licensee personnel acknowledged the inspection results presented. Licensee personnel were asked to identify any documents, materials, or information provided during the inspection that were considered proprietary. No proprietary information was identified.

1ATTACHMENT:

SUPPLEMENTAL INFORMATION

KEY POINTS OF CONTACT

Licensee

B. Hanson, Site Vice President
M. McDowell, Plant Manager
J. Cunningham, Work Management Director
R. Frantz, Regulatory Assurance Representative
P. Marcum, Electrical/I&C Design Manager
P. Simpson, Regulatory Assurance Director (Acting)
R. Peak, Site Engineering Director
O. Villireal, Nuclear Oversight
R. Weber, Senior Manager Design EngineeringNuclear Regulatory Commission
C. Pederson, Director, Division of Reactor Safety
B. Dickson, Senior Resident Inspector
D. Tharp, Resident Inspector

ITEMS OPENED, CLOSED, AND DISCUSSED

Opened, Closed, and

Discussed

None

2

LIST OF DOCUMENTS REVIEWED

The following is a list of licensee documents reviewed during the inspection, includingdocuments prepared by others for the licensee.

Inclusion on this list does not imply that NRC