IR 05000282/2007002: Difference between revisions

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| issue date = 05/14/2007
| issue date = 05/14/2007
| title = IR 05000282-07-002, 05000306-07-002, on 01/01/07 - 03/31/07; Prairie Island Nuclear Generating Plant, Units 1 and 2; Occupational Radiation Safety
| title = IR 05000282-07-002, 05000306-07-002, on 01/01/07 - 03/31/07; Prairie Island Nuclear Generating Plant, Units 1 and 2; Occupational Radiation Safety
| author name = Skokowski R A
| author name = Skokowski R
| author affiliation = NRC/RGN-III/DRP/RPB3
| author affiliation = NRC/RGN-III/DRP/RPB3
| addressee name = Palmisano T
| addressee name = Palmisano T
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=Text=
=Text=
{{#Wiki_filter:
{{#Wiki_filter:May 14, 2007Mr. Thomas PalmisanoSite Vice President Prairie Island Nuclear Generating Plant Nuclear Management Company, LLC 1717 Wakonade Drive East Welch, MN 55089SUBJECT:PRAIRIE ISLAND NUCLEAR GENERATING PLANT, UNITS 1 AND 2NRC INTEGRATED INSPECTION REPORT 05000282/2007002 AND 05000306/2007002
[[Issue date::May 14, 2007]]
 
Mr. Thomas PalmisanoSite Vice President Prairie Island Nuclear Generating Plant Nuclear Management Company, LLC 1717 Wakonade Drive East Welch, MN 55089
 
SUBJECT: PRAIRIE ISLAND NUCLEAR GENERATING PLANT, UNITS 1 AND 2NRC INTEGRATED INSPECTION REPORT 05000282/2007002 AND 05000306/2007002


==Dear Mr. Palmisano:==
==Dear Mr. Palmisano:==
Line 33: Line 28:
T. Palmisano-2-In accordance with 10 CFR 2.390 of the NRC's "Rules of Practice," a copy of this letter, itsenclosure, and your response (if any), will be available electronically for public inspection in the NRC Public Document Room or from the Publicly Available Records (PARS) component of NRC's document system (ADAMS), accessible from the NRC Web site at http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room).
T. Palmisano-2-In accordance with 10 CFR 2.390 of the NRC's "Rules of Practice," a copy of this letter, itsenclosure, and your response (if any), will be available electronically for public inspection in the NRC Public Document Room or from the Publicly Available Records (PARS) component of NRC's document system (ADAMS), accessible from the NRC Web site at http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room).


Sincerely,/RA/Richard A. Skokowski, ChiefBranch 3 Division of Reactor Projects Docket Nos. 50-282; 50-306License Nos. DPR-42; DPR-60
Sincerely,
 
/RA/Richard A. Skokowski, ChiefBranch 3 Division of Reactor Projects Docket Nos. 50-282; 50-306License Nos. DPR-42; DPR-60Enclosure:Inspection Report 05000282/2007002 and 05000306/2007002 w/Attachment: Supplemental Informationcc w/encl:D. Cooper, Senior Vice President and Chief Nuclear Officer M. Sellman, President and Chief Executive Officer Regulatory Affairs Manager J. Rogoff, Vice President, Counsel & Secretary Nuclear Asset Manager State Liaison Officer, Minnesota Department of Health Tribal Council, Prairie Island Indian Community Administrator, Goodhue County Courthouse Commissioner, Minnesota Department of Commerce Manager, Environmental Protection Division Office of the Attorney General of Minnesota
===Enclosure:===
Inspection Report 05000282/2007002 and 05000306/2007002  
 
===w/Attachment:===
Supplemental Informationcc w/encl:D. Cooper, Senior Vice President and Chief Nuclear Officer M. Sellman, President and Chief Executive Officer Regulatory Affairs Manager J. Rogoff, Vice President, Counsel & Secretary Nuclear Asset Manager State Liaison Officer, Minnesota Department of Health Tribal Council, Prairie Island Indian Community Administrator, Goodhue County Courthouse Commissioner, Minnesota Department of Commerce Manager, Environmental Protection Division Office of the Attorney General of Minnesota


=SUMMARY OF FINDINGS=
=SUMMARY OF FINDINGS=
Line 389: Line 379:


===Closed===
===Closed===
: [[Closes finding::05000282/FIN-2007002-01]]NCVFailure to Properly Control Access to a Locked HighRadiation Area
05000282/2007002-01NCVFailure to Properly Control Access to a Locked HighRadiation Area05000306/2006-002-00LERUnit 2 Event Monitoring Instrument Inoperable LongerThan Allowed by Technical Specifications05000282/2006002-02
: [[Closes LER::05000306/LER-2006-002]]-00LERUnit 2 Event Monitoring Instrument Inoperable LongerThan Allowed by Technical Specifications05000282/2006002-02
: 05000306/2006002-02URILicensee Continuing On-site Tritium Well Sample
: [[Closes finding::05000306/FIN-2006002-02]]URILicensee Continuing On-site Tritium Well Sample
Results Assessment
: Results Assessment


===Discussed===
===Discussed===
Line 400: Line 389:
==LIST OF DOCUMENTS REVIEWED==
==LIST OF DOCUMENTS REVIEWED==
The following is a list of documents reviewed during the inspection.
The following is a list of documents reviewed during the inspection.
: Inclusion on this list doesnot imply that the NRC inspectors reviewed the documents in their entirety but rather that selected sections of portions of the documents were evaluated as part of the overall inspection effort.
: Inclusion on this list doesnot imply that the NRC inspectors reviewed the documents in their entirety but rather that
: Inclusion of a document on this list does not imply NRC acceptance of the document or any part of it, unless this is stated in the body of the inspection report.
: 1R04Equipment AlignmentDiesel Generator D1Integrated Checklist C1.1.20.7-5; D2 Diesel Generator Valve Status; Revision 20Integrated Checklist C1.1.20.7-6; D2 Diesel Generator Auxiliaries and Room Cooling Local Panels; Revision 10
: Integrated Checklist C1.1.20.7-7; Diesel Generator D2 Main Control Room Switch and Indicating Light Status; Revision 13
: Integrated Checklist C1.1.20.7-8; D2 Diesel Generator Circuit Breakers and Panel Switches; Revision 1612 Component Cooling PumpIntegrated Checklist C1.1.14-1; Unit 1 Component Cooling System; Revision 23
: Diesel Generator D6Integrated Checklist C1.1.20.7-13; D6 Diesel Generator Valve Status; Revision 14Integrated Checklist C1.1.20.7-14; D6 Diesel Generator Auxiliaries and Local Panels and Switches; Revision 12
: Integrated Checklist C1.1.20.7-15; D6 Diesel Generator Main Control Room Switch and Indicating Light Status; Revision 6
: Integrated Checklist C1.1.20.7-16; D6 Diesel Generator Circuit Breakers and Panel Switches; Revision 8Complete System Alignment of the Unit 2 Safety Injection SystemIntegrated Checklist C1.1.18-2;SI,CS,CA, and HC System Checklist Unit 2; Revision 40Drawing X-HIAW-1001-6; Flow Diagram Safety Injection System Unit 2; Revision V
: Drawing X-HIAW-1001-7; Flow Diagram Safety Injection System unit 2; Revision Z
: Drawing X-HIAW-1001-8; Flow Diagram Residual Heat Removal System Unit 2;
: Revision P
: Work Request Query; All Open Unit 2 Safety Injection Work Request
: CAP 01081727; Leak Management Program Tags Do Not Appear to be Up to Date
: CAP 01002547; Repair of Boric Acid Leaks Not in Accordance with Leak Management Program
: CAP 01028606;
: WO 87305 Not On Outage Schedule
: CAP 01056608; Boric Acid Program Went from Green to Yellow
: CAP 01080095; 2SI-20-54 Has a Reoccurring Packing Leak
: CAP 01080102; 2SI-20-57 Has a Reoccurring Packing Leak
: 1R05Fire ProtectionPlant Safety Procedure F5, Appendix A; Fire Strategies for Fire Areas 25, 31, 32, 41A,41B, 81, 113, 115, and 117
: Plant Safety Procedure F5, Appendix F, Revision 20; Fire Hazard Analysis for Fire Areas 25, 31, 32, 41A, 41B, 81, 113, 115, and 117
: IPEEE
: NSPLMI-96001, Appendix B; Internal Fires Analysis; Revision 2
: 1R06External Flood ProtectionWork Order Package
: 00294373-01;SP 1293, Annual Inspection of Flood ControlMeasures Product Data Sheet No. 785; Deck-O-Seal Gun Grade Sealant
: CAP 01082159; Door 73 Missing Handle Potential Flood Concern
: CAP 01083312; Performance of SP 1293
: Work Request 21860; Door 420 Has a Loose Seal Work Request 21864; Doors MK 7, 4, and 5 Needs New Velcro Abnormal Operating Procedure
: AB-4; Flood, Revision 28
: 1R07Annual Heat Sink InspectionEngineering Calculation
: ENG-ME-604; Tube Plugging Limits for the 12 and 22 Diesel-Driven Cooling Water Pump Right Angle Drive Gear Oil Cooler; Revision 1
: Engineering Calculation
: ENG-ME-573; Tube Plugging Limits for the 12 and 22 Diesel-Driven Cooling Water Pump Jacket Water Heat Exchangers; Revision 0
: Work Order
: 297312;
: PM 3002-2-12; Revision 27
: Prairie Island Nuclear Generating Plant Form 1066; Revision 7 for the 12 Diesel-Driven Cooling Water Pump Right Angle Drive Gear Oil Cooler Prairie Island Nuclear Generating Plant Form 1066; Revision 7 for the 12 Diesel-Driven Cooling Water Pump Jacket Water Heat Exchanger
: CAP 01072185; 22
: Diesel-Driven Cooling Water Pump Gear Oil Cooler Debris Noted During Annual Preventive Maintenance
: 1R11Licensed Operator Requalification ProgramOperating Test ResultsPrairie Island Nuclear Generating Plant Licensed Operator Requalification ProgramResultsQuarterly Review of Licensed Operators' Requalification Training Simulator Evaluation Guide P9160S-001, ATT
: SQ-55, Revision 0
: 5AWI 3.15.0; Plant Operation; Revision 20
: 1R12Maintenance Effectiveness Nuclear Fuel Cladding FailuresMaintenance Rule Basis Document; Nuclear Fuel; Revision 11CAP
: 01043990; Possible Identification of a Second Fuel Leak on Unit 2
: CAP 01046466; Align Fuel Failure Investigations With Best Industry Practice
: CAP 01023855; Unit 1 Fuel Leak
: CAP 00884592; Unit 2 Fuel Leakage
: 4CAP
: 00865512; Elevated Xenon 133 in the Unit 2 PrimaryCAP
: 00826697; Unit 2 Fuel Defect Identified
: CAP 00041564; Unit 2 Fuel Defect Identified Maintenance Rule Evaluation
: 01023855-09; Unit 1 Fuel Leak Maintenance Rule Evaluation
: 000434; Unit 2 Fuel Defect Identified Maintenance Rule Expert Panel Meeting Minutes 2006-09; September 21, 2006
: Unit 1 Cycle 23 Xenon 133 Activity Unit 1 Cycle 23 Iodine Activity Unit 2 Cycle 22 and 23 Xenon 133 Activity Unit 1 Cycle 22 and 23 Iodine Activity11 Turbine-Driven Auxiliary Feedwater PumpRoot Cause Evaluation Report
: RCE 01034270-09; 11 TDAFWP [Turbine-DrivenAuxiliary Feedwater Pump] Turbine Bearing Failure
: CAP 01035021; 11 TDAFWP Trip Throttle Valve Marginally Latched
: CAP 01041666; 11 TDAFWP Trip Throttle Latch Not Fully Engaged
: CAP 01048078; 11 TDAFWP Overspeed Trip Latching Device
: CAP 01079878; 11 AFW Pump Trip Throttle Valve Latch Engagement Issues
: 1R13Maintenance Risk Assessments and Emergent Work ControlProcedure H24.1, Appendix A; Phase 1 Risk Assessment Preparation; Revision 2Unit 2 Configuration Risk Assessment for January 9, 2007
: Unit 1 Configuration Risk Assessment for January 25, 2007
: Unit 1 Configuration Risk Assessment for January 31, 2007
: Unit 2 Configuration Risk Assessment for February 7, 2007
: Unit 1 Configuration Risk Assessment for February 12, 2007
: Unit 2 Configuration Risk Assessment for February 13, 2007
: Unit 1 Configuration Risk Assessment for March 14, 2007
: Operator Logs for January 9, 2007
: Operator Logs for January 25, 2007
: Operator Logs for January 31, 2007
: Operator Logs for February 7, 2007
: Operator logs for February 12, 2007
: Operator Logs for February 13, 2007
: Operator Logs for March 14, 2007
: CAP 01070563; 121 Instrument Air Compressor Not Supported 24/7 When Maintenance Rule Red
: CAP 01070752; Bus 26 Load Sequencer Failed Surveillance SP 2095
: CAP 01076491; System Condition (Grid) Orange Not Evaluated in PRA
: 1R15Operability EvaluationsOPR 01070125CAP
: 01070125; RCP Impeller Serial Numbers Don't Match Those in Safety Analysis
: OPR 01070049CAP
: 01070049; D6 Vibration Amplitudes Exceeding Manufacturer's Limits
: 5OPR 01070752-01OPR01070752-01; Bus 26 Load Sequencer Operability EvaluationCAP
: 01070752; Bus 26 Failed Load Sequencer Surveillance SP 2095
: SP 2095; Bus 26 Load Sequencer Test; Revision 17OPR 01073261CAP
: 01073261; D2 Magnetic Drive Pump Seismic Test Different Than Installed PumpCAP
: 01073726; NRC Information Request on D2 Standby Jacket Pump
: CAP 01069591CAP
: 01069591; Abnormal Noise and Vibration Internally of 22 Main Steam IsolationValve Operational Decision-Making Issue Evaluation Document
: 1069591; 22 Main Steam Isolation Valve is Exhibiting Sounds of Metal Impacts from the Interior of the ValveOPR 01076278CAP
: 01076278; D6 Generator Axial Vibration Exceeding Vendor Limits
: 1R17Permanent Plant ModificationsEC 652; Cooling Water In-Service Test Modification; Revision 050.59 Screening No. 2670;
: EC 652; Revision 1
: 1R19Post-Maintenance TestingD1 18-Month InspectionWO Package
: 00109388-01;
: PM 3001-2-D1; Diesel Generator 24-Month InspectionWO Package
: 00294653-01;
: SP 1295: D1 Diesel Generator 6-Month Fast Start
: SP 1334; Diesel Generator 18-Month 24-Hour Load Test
: CAP 01074008; NRC Questioned Leak from D1 Inlet Air Check Valve Dashpot
: CAP 01074005; D1 Diesel Generator Standby Lube Oil System Trouble Alarm
: CAP 01074002; D1 Standby Jacket Coolant Pump Seal Leak
: CAP 01073995; D1 Opposite Side Jacket Coolant Leak
: CAP 01073453; Fuel Injector Timing Reading Different Than Last Year121 Safeguard Traveling ScreenWO
: 00286922;
: PM 3108-1-121, 121 Safeguard Traveling Screen Annual InspectionSP 1151A; Train A Cooling Water System Quarterly Test; Revision 8121 Cooling Water pump InspectionPreventive Maintenance Procedure
: PM-3107-2; 121 Cooling water Pump Inspection;Revision 25
: SP 1106C 121 Cooling Water Pump Quarterly Test; Revision 28
: CAP 01077118; 121 Motor-Driven Cooling Water Pump Performance in Action Range During
: SP 1106C
: 6D5 18-Month InspectionWO Package
: 00284064-01;
: PM-3001-2; D5 Diesel Generator 18-Month Inspection(Mechanical)
: WO Package
: 00284064-07;
: SP 2295; D5 Diesel Generator 6-Month Fast Start Test
: CAP 01078617; Fuel Injection Pump on D5 Engine 2 is Leaking
: CAP 01078575; D5 Engine 2 Fuel Rack Indicator Found Out-of-Tolerance
: CAP 01078231; Step Signed Off in D5 Inspection Prior to Completion12 Diesel Cooling Water PumpWO
: 00297312;
: PM 3002-2-12, 12 Diesel Cooling Water Pump InspectionSP 1106A; 12 Diesel Cooling Water Pump Monthly Test; Revision 6922 Main Steam Isolation ValveWO Package
: 00311170-04; Linkage Adjustment and Repack Post Maintenance TestSP 2099; Main Steam Isolation Valve Logic Test; Revision 18
: SP 2406 Main Steam Isolation Valve Inservice Test; Revision 1
: 1R20Refueling and Other Outage ActivitiesOperating Procedure 2C1.2; Unit 1 Startup Procedure; Revision 37Operating Procedure 2C1.3; Unit 1 Shutdown; Revision 58
: Unit 2 Shutdown Safety Assessment Maintenance Procedure D107; Containment Foreign Material Exclusion Control;
: Revision 2
: Maintenance Procedure 2D108; Pressurizer Power Operated Relief Valve Air Accumulator Supplementation; Revision 2
: 1R22Surveillance Testing
: SP 2307SP 2307; D6 Diesel Generator 6-Month Fast Start Test; Revision 26CAP
: 01070040; 4160 Bus Running Volts Reading Less Than Zero
: CAP 01070047; 4160 Bus Incoming Volts Reading Less Than Zero
: CAP 01070049; D6 Vibration Amplitudes Exceeding Manufacturers Limits
: SP 1334SP 1334; D1 Diesel Generator 18-Month 24-Hour Load Test; Revision 7CAP
: 01070822; Evaluate D1 EDG Cylinder Exhaust Temperatures
: CAP 01070827; D1 Diesel Generator Jacket Coolant Pump Began to Leak Following 24
: Hour Run
: CAP 01070830; D1 EDG Standby Lube Oil System Trouble Alarm
: SP 1089ASP 1089A; Train A RHR Pump and Suction Valve from Refueling Water Storage Tank Quarterly Test; Revision 10
: CAP 01076783; Steps in
: SP 1106 Marked as NA Incorrectly
: CAP 01079787; Quarterly Requirements of
: SP 1102 Not Performed
: CAP 01080814; Missed Surveillance and Near Misses Apparent Cause Evaluation
: 01080814-04; Missed Surveillance and Near Misses
: SP 1106BSP 1106B; 22 Diesel Cooling Water Pump Monthly Test; Revision 66CAP
: 01077480; 22 DDCLP Starting Time Was Outside the Expected Range
: SP 2405SP 2405; Unit 2 Mid-Cycle and Refueling Outage Boric Acid Corrosion ExaminationInside Containment; Revision1
: CAP 01062028; Section XI Relevant Leak on MV-32233
: CAP 01079969; Boric Acid Leak on 2RC-1-17
: CAP 01080001; 2RC-195-14 Boric Acid Packing Leak
: CAP 01080022; 2RC-195-11 Has Packing Leak
: CAP 01080059;
: MV-32169 Boddy to Bonnet Leak
: CAP 01080061; Boric Acid Work Request Inappropriately Closed
: CAP 01080076; Packing Leak on MV-32173
: CAP 01080086; ASME Section XI, Relevant Boric Acid Leak on 2FT-415
: CAP 01080087;
: CV-31462 Has a Reoccurring Packing Leak
: CAP 01080095; 2SI-20-54 Has a Reoccurring Packing Leak
: CAP 01080102; 2SI-20-57 Has a Reoccurring Packing Leak
: CAP 01080104; Packing Leak on MV-32170
: CAP 01080116; ASME Section XI, Relevant Boric Acid Leak on 2FT-428
: CAP 01080117; ASME Section XI, Relevant Boric Acid Leak on 2FT-427
: CAP 01080119; ASME Section XI, Relevant Boric Acid Leak on 2FT-426
: SP 2371WO
: 315425;
: SP 2371 Cold Shutdown Test of Residual Heat Removal Pumps andCheck Valves Engineering Calculation
: ENG-ME-546; Westinghouse Calculation Note CCN-SEE-02-
: 90, Residual Heat Removal and Safety Injection Flow Rates for Loss of Coolant Accident Mass and Energy Release and Containment Analysis; Revision 0Procedure H10.1; ASME Inservice Testing Program; Revision 20
: CAP 01080132; Residual Heat Removal Pump Outside Inservice Test Action Range
: 1R23Temporary ModificationsEC 9802; Install Seal on the Snubber for
: CV-31135, Feedwater to 21 Steam GeneratorWO
: 00309614; U2,
: CV-31135, Actuator Has Oil Leak
: CAP 01068662; Feedwater to 21 Steam Generator CV Has Oil Leak on Damper
: CAP 01070449; O-Ring Came Out of T-MOD on CV-31135
 
==1EP6 Drill EvaluationEmergency Plan Exercise Manual; Revision 0Prairie Island Nuclear Generating Plant February 6, 2007,==
: EP Drill Critique Report
: CAP 01075781; ERO Drill Did Not Correctly Activate the TSC
: CAP 01075820; E-Plan Response vehicles Difficult to Enter
: CAP 01075844; EAL Gum Label
: SS1.1 Has 10 Minutes Instead of 15 Minutes
: CAP 01076073; E-Plan Field Team Vehicles Pre-staged
: CAP 01076121; Conduct of Drill Issues Identified During 2/6/07 Drill
: 8CAP
: 01076125; Failed Demonstration Criteria A01, Number 3 in TSC, OSC, and EOFCAP
: 01076132; Drill Objective B3 Was Failed During the February 6, 2007, EP Drill
: CAP 01076141; New Motorola Portable Radios Did Not Operate Properly
: CAP 01076217; PITC PA System Inoperable Speakers
: CAP 01076348; Lack of Attention to Detail in EP Drill Critique Reports
: CAP 01076362; Failure to Follow Requirements - Completion of EP Staff Training
: CAP 01076363; Incorrect Revision of Form Used for Documenting Objectives
: CAP 01076365; Untimely Completion of EP Drill Critique Reports
: CAP 01076366; Dose Assessment Not Designated as Key Demonstration Criteria
: CAP 01076458; Negative Trend - ERO Performance in Command and Control2OS2ALARA Planning and ControlsCAP
: 1032220; Locked High Radiation Area Barrier to Spent Resin Tank Area Found Unsecured
: CAP 1033802; Adverse Trend High Radiation Area Control (1R24)
: CAP 1066716; Contamination in The Clean Area of The U1 CS Pump Room
: CAP 1066929; HRA Identified at 123/124 ADT Filters; dated December 11, 2006
: CAP 1071917; NOS Identified Issues with Monthly PI Data Validation Techniques Door Transaction History (Doors 100 and 274)
: Passport Dose Histories; Selected Individuals; dated December 4, 2006
: Radiation Protection/Chemistry Lessons Learned 2R24 Feedback; draft
: 1R24 Post-Outage ALARA Report; undated
: 2R24 Post-Outage RWP/Work Order Dose Summary Reports; dated February 7, 2007
: PINGP 438; Radioactive Waste Container Log Sheet; Revision 12
: PINGP 1016; High Radiation Area or Locked HRA Key Issue; Revision 10
: PINGP 1287; ALARA Planning Checklist; Revision 4
: PINGP 1470; High Radiation Area/Locked High Radiation Area Entry and Control Briefing Sheet; Revision 3; August 4, 2004; Revision 4; October 4, 2006; and Revision
: 5; dated November 14, 2006
: C21.1.3.1-1; Liquid Waste Disposal System; Revision 0
: C21.1-6.1; Processing Chemical Drain Tank; Revision 3
: C21.1-6.21A; Transferring Non-Aerated Drains Sump Tank to CVCS Holdup Tanks;
: Revision 6
: C21.1-6.4; Processing Miscellaneous Drains; Revision 2
: FP-PA-ARP-01; CAP Action Request Process; Revision 14
: FP-RP-JPP-01; Radiation Protection Job Planning; Revisions 1 and 2
: FP-RP-RWP-01; Radiation Work Permit; Revision 5
: FP-RP-SD-01; Special Dosimetry; Revision 1
: FP-WM-OVW-01; Work Management Process Overview; Revision 0
: FP-WM-PLA-01; Work Order Planning Process; Revision 1
: RPIP 1000; Radiation Protection Implementing Procedure Control; Revision 13
: RPIP 1001; Radiation Protection Program; Revision 8
: RPIP 1004; Radiation Protection ALARA Program; Revision 6
: RPIP 1008; Radiation Protection Key Control; Revision 7
: RPIP 1008; Radiation Protection Key Control; Revision 8
: RPIP 1106; Access Control Procedures; Revision 15
: RPIP 1110; Administrative Dose Controls; Revision 17
: RPIP 1120; Posting of Restricted Areas; Revision 26
: 9RPIP 1135; RWP Coverage; Revision 18RPIP 1311; Resin Liner / PDV Control; Revision 12
: RPIP 1318; Dewatering Filter Elements in High Integrity Containers; Revision 4
: RPIP 1721; Resin Sluice; Revision 16
: QF 1203; Radiological Work Assessment Form;
: WOs 303846, 303862,
: 303863/1,2,3,4,5,6,7; dated November 09, 2006
: QF 1205; Radiological Work Assessment Form - Exposure Controls; WOs 303846,
: 303862, 303863/1,2,3,4,5,6,7; dated November 10, 2006
: QF 1209; Radiological Pre-Job Briefing Form;
: WOs 303846, 303862,
: 303863/1,2,3,4,5,6,7; undated
: WO 8836; Replace Wooden Door with Metal Door (IR 1032220); dated August 29, 2006
: WO 155062; Incore Drives; Revision 1
: WO 154846; Containment Inspections; Revision 01-05
: WO 154920; Insulation Removal; Revision 1
: Work Plan
: 303862; Transfer Resin Liner 129 to the Shipping Cask; undated
: 5AWI 3.1.0; Site Organization and General Responsibilities; Revision 17
: 5AWI 10.1.0; Radiation Protection Program; Revision 7
: 5AWI 10.1.3; Station ALARA Committee; Revision 5
: 5AWI 10.11.6; Pre-Job Brief; Revision 10
: 5AWI 10.11.7; Post-Job Critique; Revision 54OA1Performance Indicator VerificationScrams, Scrams With Loss of Normal Heat Removal, and Unplanned Power ChangesPrairie Island Nuclear Generating Plant Form 1318A; Performance Indicators-InitiatingEvents; Revision 0 for 1
st Quarter 2006, 2
nd Quarter 2006, 3
rd Quarter 2006,4th Quarter 2006; Unit 1 and Unit 2.
: Plant Procedure H33; Performance Indicator Reporting; Revision 6
: Section Work Instruction O-53; Operations Performance Indicator Reporting; Revision 1
: Unit 1 and 2 Operating Logs for January 1, 2006, through December 31, 2006
: CAP01073196; 121 Cooling Water Line Segment Unavailability Not Calculated Correctly4OA2Identification and Resolution of ProblemsCAP
: 01070049; D6 Vibration Amplitudes Exceeding Manufacturer's LimitsCAP
: 01076278; D6 EDG Generator Axial Vibration Exceeding Vendor Limits4OA3Event FollowupCAP
: 01063645; Unit 2 2N52 in Containment Cable IssuesCAP
: 01063965; 2N51 Raychem Found to be Inadequate
: 10
==LIST OF ACRONYMS==
USEDADAMSAgencywide Documents Access and Management SystemALARAAs-Low-As-Is-Reasonably-Achievable
ASMEAmerican Society of Mechanical Engineers
CAPCorrective Action Program Action Request
CFRCode of Federal Regulations
DDCLPDiesel-Driven Cooling Water Pump
HICHigh Integrity Container
HRAHigh Radiation Area
HXHeat Exchanger
IMCInspection Manual Chapter
IPEEEIndividual Plant Examination of External Events
IRInspection Report
LERLicensee Event Report
LHRALocked High Radiation Area
mRem/hrmillirem per hour
NCVNon-Cited Violation
NRCU.S. Nuclear Regulatory Commission
OPROperability Recommendation
PARSPublicly Available Records
PIPerformance Indicator
RHRResidual Heat Removal
RPRadiation Protection
RWPRadiation Work Permit
SDPSignificance Determination Process
SPSurveillance Procedure
TSTechnical Specifications
URIUnresolved Item
USARUpdated Safety Analysis Report
: [[WOW]] [[ork Order]]
}}
}}

Revision as of 00:20, 13 July 2019

IR 05000282-07-002, 05000306-07-002, on 01/01/07 - 03/31/07; Prairie Island Nuclear Generating Plant, Units 1 and 2; Occupational Radiation Safety
ML071340358
Person / Time
Site: Prairie Island  Xcel Energy icon.png
Issue date: 05/14/2007
From: Richard Skokowski
NRC/RGN-III/DRP/RPB3
To: Thomas J. Palmisano
Nuclear Management Co
References
FOIA/PA-2010-0209 IR-07-002
Download: ML071340358 (39)


Text

May 14, 2007Mr. Thomas PalmisanoSite Vice President Prairie Island Nuclear Generating Plant Nuclear Management Company, LLC 1717 Wakonade Drive East Welch, MN 55089SUBJECT:PRAIRIE ISLAND NUCLEAR GENERATING PLANT, UNITS 1 AND 2NRC INTEGRATED INSPECTION REPORT 05000282/2007002 AND 05000306/2007002

Dear Mr. Palmisano:

On March 31, 2007, the U. S. Nuclear Regulatory Commission (NRC) completed an integratedinspection at your Prairie Island Nuclear Generating Plant, Units 1 and 2. The enclosed report documents the inspection findings which were discussed on April 4, 2007, with you and other members of your staff. This inspection examined activities conducted under your license as they relate to safety and tocompliance with the Commission's rules and regulations and with the conditions of your license.

The inspectors reviewed selected procedures and records, observed activities, and interviewed personnel.Based on the results of this inspection, one NRC identified finding of very low safetysignificance was identified. This finding was determined to involve a violation of NRC requirements. However, because of its very low safety significance, and because the issue was entered into your corrective action program, the NRC is treating the issue as a Non-Cited Violation (NCV) in accordance with Section VI.A.1 of the NRC's Enforcement Policy.If you contest any finding or the subject/severity of any Non-Cited Violation in this report, youshould provide a response within 30 days of the date of this inspection report, with the basis for your denial, to the U.S. Nuclear Regulatory Commission, ATTN: Document Control Desk, Washington DC 20555-0001, with a copy to the Regional Administrator, U.S. Nuclear Regulatory Commission - Region III, 2443 Warrenville Road, Suite 210, Lisle, IL 60532-4352;the Director, Office of Enforcement, U. S. Nuclear Regulatory Commission, Washington, DC 20555-0001; and the NRC Resident Inspector Office at the Prairie Island facility.

T. Palmisano-2-In accordance with 10 CFR 2.390 of the NRC's "Rules of Practice," a copy of this letter, itsenclosure, and your response (if any), will be available electronically for public inspection in the NRC Public Document Room or from the Publicly Available Records (PARS) component of NRC's document system (ADAMS), accessible from the NRC Web site at http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room).

Sincerely,

/RA/Richard A. Skokowski, ChiefBranch 3 Division of Reactor Projects Docket Nos. 50-282; 50-306License Nos. DPR-42; DPR-60Enclosure:Inspection Report 05000282/2007002 and 05000306/2007002 w/Attachment: Supplemental Informationcc w/encl:D. Cooper, Senior Vice President and Chief Nuclear Officer M. Sellman, President and Chief Executive Officer Regulatory Affairs Manager J. Rogoff, Vice President, Counsel & Secretary Nuclear Asset Manager State Liaison Officer, Minnesota Department of Health Tribal Council, Prairie Island Indian Community Administrator, Goodhue County Courthouse Commissioner, Minnesota Department of Commerce Manager, Environmental Protection Division Office of the Attorney General of Minnesota

SUMMARY OF FINDINGS

IR 05000282/2007002, 05000306/2007002; 01/01/07 - 03/31/07; Prairie Island NuclearGenerating Plant, Units 1 and 2; Occupational Radiation Safety.This report covers a 3-month period of baseline resident inspection and announced baselineinspection of the operator requalification program and occupational radiation protection. The inspection was conducted by the resident inspectors and inspectors from the Region III office. The inspectors identified one finding and associated Non-Cited Violation. The significance ofmost findings is indicated by their color (Green, White, Yellow, Red) using Inspection Manual Chapter (IMC) 0609, "Significance Determination Process" (SDP). Findings for which the SDP does not apply may be "Green" or be assigned a severity level after NRC management review.

The NRC's program for overseeing the safe operation of commercial nuclear power reactors is described in NUREG-1649, "Reactor Oversight Process," Revision 3, dated July 2000.A.Inspector-Identified and Self-Revealed Findings

Cornerstone: Occupational Radiation Safety

Green.

A finding of very low safety significance and associated Non-Cited Violation wasinspector-identified during review of an issue where a station operator entered into a Locked High Radiation Area (LHRA) without authorization while a high integrity container was being moved to the radioactive waste barrel yard. The licensee has entered this finding into the corrective action program. The finding was more than minor because it was associated with the Program/Processattribute of the Occupational Radiation Safety cornerstone, and potentially affected the cornerstone objective to ensure adequate protection of worker health and safety from exposure to radiation. The finding was determined to be of very low safety significance because the finding did not involve As-Low-As-Reasonably-Achievable planning,collective dose was not a factor, it did not involve an overexposure, and the individual involved received very low dose. Additionally, there was not a substantial potential for a worker overexposure, and the licensee's ability to assess worker dose was not compromised. The initial licensee evaluation of this issue was inadequate because it failed to addressthis event in relationship to previous similar events concerning the performance and effectiveness of LHRA guards. Specifically, Prairie Island had a similar event involving the performance of LHRA guards controlling access to radiologically significant areas during its April 2006 refueling outage. Had the previous event been properly identified, entered into the licensee's corrective action program, and evaluated adequately and in a timely manner, this December 2006 event may not have occurred. Consequently, this finding also related to the cross-cutting area of problem identification and resolution dealing with the corrective action program component to ensure issues are promptly identified and fully evaluated to allow timely corrective actions. (Section 2OS1)

B.Licensee-Identified Violations

None.

2

REPORT DETAILS

Summary of Plant StatusUnit 1 operated at or near full power throughout the inspection period.Unit 2 operated at or near full power until January 4, 2007, when power was reduced to about98 percent to perform maintenance on the feed water control system. Full power was restored on January 5, 2007. The unit remained at full power until February 28, 2007, when the unit was shut down for a maintenance outage (2F2401) to repair the 22 main steam isolation valve. The reactor was restarted and the generator placed on-line on March 8, 2007. Unit 2 achieved full power on March 13, 2007, and operated at or near full power for the remainder of the inspection period.1.REACTOR SAFETYCornerstone: Initiating Events, Mitigating Systems, and Barrier Integrity1R04Equipment Alignment (71111.04Q and S)

.1 Partial Walkdowns

a. Inspection Scope

The inspectors performed three partial system equipment alignment inspection samplescomprised of in-plant walkdowns of accessible portions of trains of risk-significant equipment associated with the mitigating systems cornerstone. The inspectors conducted the inspections during times when the trains were of increased importance due to the redundant trains or other related equipment being unavailable. The inspectors also reviewed documents entering deficient conditions associated with equipment alignment issues into the corrective action program verifying that the licensee was identifying issues at an appropriate threshold and entering those issues into their corrective action program in accordance with the licensee's corrective action procedures.The inspectors utilized the valve and electric breaker checklists, where applicable, toverify that the components were properly positioned and that support systems were lined up as needed. The inspectors also examined the material condition of the components and observed operating parameters of equipment to verify that there were no obvious performance deficiencies. The inspectors reviewed outstanding work orders (WOs) and corrective action program documents (CAPs) associated with the operable trains to verify that those documents did not reveal issues that could affect the completion of the available train's safety functions. The inspectors used the information in the appropriate sections of the Technical Specifications (TS) and the Update Safety Analysis Report (USAR) to determine the functional requirements of the systems.The inspectors verified the alignment of the following trains:

3*diesel generator D2 while D1 was out of service for planned maintenance onJanuary 23, 2007;*12 component cooling pump while the 11 component cooling pump was out ofservice for planned maintenance on January 31, 2007; and *diesel generator D6 while D5 was out of service for planned maintenance onFebruary 21, 2007.Key documents used by the inspectors in conducting this inspection are listed in theAttachment to this report.

b. Findings

No findings of significance were identified.

.2 Complete System Alignment Walkdown of Unit 2 Safety Injection System

a. Inspection Scope

During the week of March 5, 2007, the inspectors performed a detailed in-plantwalkdown of the alignment and condition of the Unit 2 safety injection system. The safety injection system is a risk-significant and safety-related mitigating system that provides water inventory to the reactor coolant system during off-normal and accident conditions. The inspectors also reviewed CAPs associated with equipment alignment issues to verify that the licensee was identifying issues at an appropriate threshold and entering them into their corrective action program in accordance with the licensee's corrective action procedures.The inspectors used applicable alignment checklists and plant drawings to verify thatsystem components were properly positioned to support the completion of system safety functions and to verify that the as-found system configuration matched the configuration specified in the system alignment checklists and plant drawings. The inspectors examined the material condition of the components, such as pumps, supports and snubbers, motors, valves, instrumentation, controls, bus relays, and electrical panels.

Where applicable, the inspectors examined outstanding design issues, temporary modifications, and operator workarounds. Where applicable, the inspectors verified that tagging clearances were appropriate and attached to the specified equipment. The inspectors reviewed outstanding WOs, Work Requests, and CAPs associated with the trains to determine if any degraded conditions existed that could affect the accomplishment of the system's safety functions. The inspectors referred to the TS, USAR, and other design basis documents to determine the functional requirements of the systems and verified those functions could be performed if needed. Key documents used by the inspectors in conducting this inspection are listed in the Attachment to this inspection report. This inspection effort constituted one complete system alignment inspection sample fora system associated with the mitigating systems cornerstone.

b. Findings

No findings of significance were identified.

1R05 Fire Protection (71111.05)

.1 Quarterly Fire Protection Area Walkdowns

a. Inspection Scope

The inspectors conducted in-office and in-plant reviews of portions of the licensee's FireHazards Analysis and Fire Strategies to verify consistency between those documents and the as-found configuration of the installed fire protection equipment and features in the fire protection areas listed below. The inspectors selected fire areas for inspection based on their overall contribution to internal fire risk as documented in the Individual Plant Examination of External Events (IPEEE), potential to impact equipment which could initiate a plant transient, or impact on the plant's ability to respond to a security event. The inspectors assessed the control of transient combustibles and ignition sources, the material and operational condition of fire protection systems and equipment, and the status of fire barriers. In addition, the inspectors reviewed CAPs associated with fire protection issues to verify that the licensee was identifying issues at an appropriate threshold and entering them into their corrective action program in accordance with the licensee's corrective action procedures. The following nine fire areas were inspected by in-plant walkdowns supporting thecompletion of nine fire protection zone walkdown samples:*Fire Area 25, diesel generator D1 room on January 16, 2007;*Fire Area 31, east auxiliary feedwater pump room on January 16, 2007;

  • Fire Area 81, bus 16 switchgear room on January 17, 2007;
  • Fire Area 113, diesel generator D5 day tank room on January 17, 2007;
  • Fire Area 115, diesel generator D5 lubricating oil make-up tank room onJanuary 17, 2007;*Fire Area 117, bus 25 switchgear room on January 17, 2007;
  • Fire Area 41A, plant screenhouse 670-foot elevation on January 18, 2007; and
  • Fire Area 41B, cooling water pump and safeguard traveling screen rooms onJanuary 18, 2007.Key documents used by the inspectors in conducting this inspection are listed in theAttachment to this inspection report.

b. Findings

No findings of significance were identified.

51R06Flood Protection Measures (71111.06)

a. Inspection Scope

The inspectors performed an in-office review of the most recently completedsurveillance procedure (SP) for the inspection of plant flooding barriers and the abnormal operating procedure for flooding. The contents of these documents were compared to the plant flood protection design sections in the USAR and the assumption contained in the IPEEE associated with an external flooding event. This inspection effort completed the annual external flood protection inspection sample under the initiating events cornerstone.The inspectors performed an in-plant inspection of flood protection barriers in theauxiliary building, turbine building, D5/D6 diesel generator building, and the old screenhouse comparing the as-found conditions of the flood protection panels against the acceptance criteria in the SP. The inspectors also verified that the actions specified in the abnormal operating procedure for flooding could be performed in a timely manner (three days), if required, and the necessary hardware and consumable materials were available and still within the usable shelf life. The inspectors reviewed several CAPs and Work Requests to verify that minordeficiencies identified during this inspection were entered into the licensee's corrective action program; that problems associated with plant equipment relied upon to prevent or minimize flooding were identified at an appropriate threshold; and that corrective actions commensurate with the significance of the issue were identified and implemented. As part of this inspection, the inspectors reviewed the documents listed in the Attachment.

b. Findings

No findings of significance were identified.

1R07 Heat Sink Performance (71111.07)

a. Inspection Scope

On February 26, 2007, the inspectors observed the licensee's inspection of the followingsafety-related heat exchangers:*12 diesel-driven cooling water pump (DDCLP) jacket water heat exchanger (HX);

and*12 DDCLP right angle gear drive lubricating oil cooler.These heat exchangers were selected for review because the cooling water system wasranked high in the plant specific risk assessment and functions to support the proper operation of nearly all safety-related mitigating systems and provided the plant's connection to the ultimate heat sink. This inspection effort completed one heat sink inspection procedure sample under the mitigating systems cornerstone.

6The inspectors performed an independent as-found inspection of the HXs associatedwith the 12 DDCLP immediately after their opening and discussed the as-found condition of the HXs with the system engineer and the Generic Letter 89-13 program engineer. The inspectors reviewed the completed work package for the inspection and cleaning of the 12 DDCLP jacket water and right angle gear drive lubricating oil HXs comparing the as-found condition to the applicable tube plugging calculation acceptance criteria. The inspectors reviewed Procedure H21, "Generic Letter 89-13 Implementing Program," Revision 10, governing Generic Letter 89-13 heat exchanger inspections in order to verify that the licensee was properly implementing their program. The inspectors also reviewed CAPs to verify that the licensee was identifying issues atan appropriate threshold and entering them into their corrective action program in accordance with licensee's corrective action procedures. Key documents used by the inspectors in conducting this inspection are listed in the Attachment to this report.

b. Findings

No findings of significance were identified.

1R11 Licensed Operator Requalification (71111.11)

.1 Operating Test Results

a. Inspection Scope

The inspectors reviewed the overall pass/fail results of the comprehensive annual jobperformance measure operating tests and the annual simulator operating tests (required to be given per 10 CFR 55.59(a)(2)). The operating tests were administered by the licensee from August 2006 through October 2006. The overall results were compared with the Significance Determination Process (SDP) in accordance with NRC Inspection Manual Chapter (IMC) 0609, Appendix I, "Operator Requalification Human Performance Significance Determination Process." Key documents used by the inspectors in conducting this inspection are listed in the Attachment to this inspection report.

b. Findings

No findings of significance were identified.

.2 Quarterly Review of Licensed Operators' Requalification Training

a. Inspection Scope

On January 22, 2007, the inspectors performed a quarterly review of licensed operatorrequalification training in the simulator, which constituted one licensed operator requalification inspection sample. The inspectors observed a crew during an evaluated exercise in the plant's simulator facility. The inspectors compared crew performance to licensee management expectations. The inspectors verified that the crew completed all of the critical tasks for each exercise scenario. For any weaknesses identified, the 7inspectors observed that the licensee's evaluators noted the weaknesses and discussedthem in the critique at the end of the session.The inspectors assessed the licensee's effectiveness in evaluating the requalificationprogram ensuring that licensed individuals would operate the facility safely and within the conditions of their licenses, and evaluated licensed operator mastery of high-risk operator actions. The inspection activities included, but were not limited to, a review of high-risk activities, emergency plan performance, incorporation of lessons learned, clarity and formality of communications, task prioritization, timeliness of actions, alarm response actions, control board operations, procedural adequacy and implementation, supervisory oversight, group dynamics, interpretations of TS, simulator fidelity, and licensee critique of performance. Key documents used by the inspectors in conducting this inspection are listed in theAttachment to this inspection report.

b. Findings

No findings of significance were identified.

1R12 Maintenance Effectiveness

(71111.12)

.1 Routine Maintenance Effectiveness

a. Inspection Scope

The inspectors reviewed repetitive maintenance activities to assess maintenanceeffectiveness, including Maintenance Rule (10 CFR 50.65) activities, work practices, and common cause issues. The inspectors performed two issue/problem-oriented maintenance effectiveness samples under the mitigating systems and barrier integrity cornerstones. The inspectors assessed the licensee's maintenance effectiveness associated with problems on: *nuclear fuel cladding failures; and*11 turbine-driven auxiliary feedwater pump turbine bearing failure and overspeedtrip throttle latch mechanism engagement on March 8, 2007.The inspectors conducted in-office reviews of the licensee's maintenance ruleevaluations of equipment failures for maintenance preventable functional failures and equipment unavailability time calculations, comparing the licensee's evaluation conclusions to applicable Maintenance Rule (a)(1) performance criteria. Additionally, the inspectors reviewed scoping, goal-setting (where applicable), performance monitoring, short-term and long-term corrective actions, functional failure definitions, and current equipment performance status.The inspectors reviewed CAPs for significant equipment failures associated with risk-significant and safety-related mitigating equipment to ensure that those failures were properly identified, classified, and corrected. The inspectors reviewed other CAPs to assess the licensee's problem identification threshold for degraded conditions, the 8appropriateness of specified corrective actions, and that the timeliness of theimplementation of corrective actions were commensurate with the safety significance of the identified issues. Key documents used by the inspectors in conducting this inspection are listed in the Attachment to this report.

b. Findings

No findings of significance were identified.

1R13 Maintenance Risk Assessments and Emergent Work Control (71111.13)

a. Inspection Scope

The inspectors reviewed the licensee's management of plant risk during emergentmaintenance activities or during activities where more than one significant system or train was unavailable. The activities were chosen based on their potential impact on increasing the probability of an initiating event or impacting the operation of safety-significant equipment. The inspections were conducted to determine whether evaluation, planning, control, and performance of the work were done in a manner to reduce the risk and minimize the duration where practical, and that contingency plans were in place where appropriate.The licensee's daily configuration risk assessment records and observations of work inprogress were used by the inspectors to verify that the equipment configurations were properly listed, protected equipment were identified and were being controlled where appropriate, work was conducted properly, and significant aspects of plant risk were communicated to the necessary personnel. The inspectors verified that minor issues identified during the inspection were entered into the licensee's corrective action program.In addition, the inspectors reviewed selected issues, listed in the Attachment, that thelicensee encountered during the activities, to determine whether problems were entered into the corrective action program with the appropriate characterization and significance.The inspectors completed seven samples under the initiating events and mitigatingsystems cornerstones by reviewing the following activities:*the emergent failure of bus 26 load sequencer with the planned unavailability ofthe 121 instrument air compressor, the 12 condensate pump, 13 charging pump, and D1 diesel generator on January 9, 2007;*the planned unavailability of diesel generator D1, 21 component cooling pump,and the 121 instrument air compressor on January 25, 2007;*the planned unavailability of the 121 intake bypass gate, the 121 safeguardstraveling screen, and the 11 component cooling pump on January 31, 2007;*the planned unavailability of volume control tank level transmitter LT-112,122 intake bypass gate, and the 21 charging pump on February 7, 2007;*the planned unavailability of the 122 intake bypass gate, D2 diesel generator,121 motor-driven cooling water pump, bus 27, and the Red Rock 2 transmission line; 9*the planned unavailability of the 122 intake bypass gate, the Red Rock 2transmission line, and breaker 2RSY on February 13, 2007; and*the planned unavailability of the 122 instrument air compressor, the 13 chargingpump, the 12 component cooling pump, the Byron transmission line, and the Red Rock 2 transmission line on March 14, 2007.

b. Findings

No findings of significance were identified.

1R15 Operability Evaluations (71111.15)

a. Inspection Scope

The inspectors reviewed the technical adequacy of six operability evaluationscompleting six operability evaluation inspection samples associated with equipment performance under the initiating events, mitigating systems, and barrier integrity cornerstones. The inspectors conducted these inspections by in-office review of associated documents and in-plant walkdowns of affected areas and plant equipment. The inspectors compared degraded or nonconforming conditions of risk-significantstructures, systems, and components associated with barrier and mitigating systems and against the functional requirements described in the TS, USAR, and other design basis documents; determined whether compensatory measures, if needed, were implemented; and determined whether the evaluation was consistent with the requirements of Administrative Work Instruction 5AWI 3.15.5, "Operability Determinations." The following operability evaluations were reviewed by inspectors:*Operability Recommendation (OPR) 01070125 that documented the operabilityof the reactor coolant pumps with impellers that had different serial numbers than those used in the safety analysis for core design, loss of coolant accident, loss of reactor coolant system flow, steam line break, and fuel assembly hold down;*OPR 01070049 that documented the operability of emergency diesel generatorD6 with generator axial vibration greater than the manufacturer's recommendation;*OPR 01070752-01 that documented the operability of the bus 26 load sequencerfollowing receipt of an unexpected error code during testing;*OPR 01073261 that documented the operability of emergency diesel generatorD2 with a standby jacket coolant pump impeller that was a different size than was used for seismic qualification;*CAP 01069591 prompt operability determination for the abnormal noise andvibration exhibited by the 22 main steam isolation valve; and*OPR 01076278 that documented the operability of emergency diesel generatorD6 with generator bearing vibration exceeding vendor limits on February 12, 2007.Key documents used by the inspectors in conducting this inspection are listed in theAttachment to this inspection report.

b. Findings

No findings of significance were identified.

1R17 Permanent Plant Modifications (Annual) (71111.17)

a. Inspection Scope

The inspectors evaluated Design Change EC 652, "Cooling Water In-Service TestModification." The modification added flow meters/transmitters in the piping that supplies cooling water to the diesel-driven cooling water pump diesel jacket and pressure transmitters on the pump discharge piping. These instruments were added to address a concern regarding unmonitored flow paths which did not comply with American Society of Mechanical Engineers (ASME) Code requirements for in-service testing. The inspectors' effort completed one permanent plant modification inspection

sample.The inspectors reviewed the modification installed in March 2007 to verify that thedesign basis, licensing basis, and performance capability of risk-significant systemswere not degraded by the installation of the modification. The inspectors considered the design adequacy of the modification by performing a review of the modification's impact on licensing basis (10 CFR 50.59), flow paths, plant electrical requirements, equipment protection, operation, failure modes, and other related process requirements. The inspectors conducted this inspection by review of documents and in-plant walkdowns of associated plant equipment. Key documents used by the inspectors in conducting this inspection are listed in theAttachment to this inspection report.

b. Findings

No findings of significance were identified.

1R19 Post-Maintenance Testing (71111.19)

a. Inspection Scope

The inspectors assessed post-maintenance testing completing six post-maintenancetest inspection samples. The inspectors selected post-maintenance tests associated with important mitigating and barrier integrity systems to ensure that the testing was performed adequately, demonstrated that the maintenance was successful, and that operability of associated equipment and/or systems was restored. The inspectors conducted these inspections by in-office review of documents, in-plant walkdowns of associated plant equipment, and interviews with responsible personnel. The inspectors observed and assessed the post-maintenance testing activities for the following maintenance activities:*D1 diesel generator 18-month inspection on January 25, 2007; 11*121 safeguard traveling screen following preventive maintenance onJanuary 30, 2007;*121 motor-driven cooling water pump inspection on February 13, 2007;

  • D5 diesel generator 18 month inspection on February 20, 2007;
  • 12 diesel cooling water pump following preventive maintenance onFebruary 28, 2007; and *22 main steam isolation valve packing replacement and actuator adjustment onMarch 8, 2007.The inspectors reviewed the appropriate sections of the TS, USAR, and maintenancedocuments to determine the systems' safety functions and the scope of the maintenance. The inspectors also reviewed CAPs to verify that the licensee was identifying issues at an appropriate threshold and entering them into their corrective action program in accordance with the licensee's corrective action procedures. Key documents used by the inspectors in conducting this inspection are listed in the to this report.

b. Findings

No findings of significance were identified.

1R20 Refueling and Other Outage Activities

a. Inspection Scope

The inspectors observed the licensee's performance during a planned Unit 2maintenance outage (2F2401) conducted between February 28, 2007, and March 8, 2007. The purpose of the outage was to repair the 22 main steam isolation valve. These inspection activities represent one outage inspection sample.This inspection consisted of an in-office review of the licensee's outage schedule,safe shutdown plan, and procedures governing the outage. Specifically, the inspectors assessed whether the licensee planned to effectively manage elements of shutdown risk pertaining to reactivity control, decay heat removal, inventory control, electrical power availability, and containment integrity. Key documents used by the inspectors in conducting this inspection are listed in the Attachment to this report. The inspectors conducted in-plant observations of the following outage activities daily:

  • attended outage management turnover meetings to verify that the currentshutdown risk status was accurate, well understood, and adequately communicated;*performed walkdowns of the main control room to observe the alignment ofsystems important to shutdown risk; and*performed walkdowns to observe ongoing work activities and foreign materialexclusion control.

12The inspectors performed in-plant observations of the following specific activities: *shutdown safety assessment;*plant cooldown;

  • plant start up and power ascension.

b. Findings

No findings of significance were identified.

1R22 Surveillance Testing (71111.22)

a. Inspection Scope

During this inspection period, the inspectors completed six surveillance inspectionsamples. Observation of surveillance procedures SP 1089A and SP 2371 completed the quarterly inservice testing inspection sample requirement of a risk-significant pump or valve surveillance test. The observation of SP 2405 completed the requirement inspection sample to observe a reactor coolant system leakage integrity test sample.

The inspectors selected the following surveillance testing activities as samples:*SP 2307, D6 Diesel Generator 6-Month Fast Start Test on January 4, 2007;*SP 1334; D1 Diesel Generator 18-Month 24-Hour Load Test on January 8, 2007;

  • SP 1089A; Train A Residual Heat Removal (RHR) Pump and Suction Valve fromRefueling Water Storage Tank Quarterly Test on February 1, 2007;*SP 1106B; 22 Diesel Cooling Water Pump Monthly Test on February 15, 2007;
  • SP 2405; Unit 2 Mid-Cycle and Refueling Outage Boric Acid CorrosionExaminations Inside Containment on February 28, 2007; and*SP 2371; Cold Shutdown Test of RHR Pumps and Check Valves onMarch 4, 2007.During completion of the inspection samples, the inspectors observed in-plant activitiesand reviewed procedures and associated records to verify, when applicable, that:* preconditioning did not occur;* effects of the testing had been adequately addressed by control room personnelor engineers prior to the commencement of the testing;* acceptance criteria was clearly stated, demonstrated operational readiness, andwas consistent with the system design basis;* plant equipment calibration was correct, accurate, properly documented, and thecalibration frequency was in accordance with TS, USAR, procedures, and applicable commitments;* measuring and test equipment calibration was current;
  • test equipment was used within the required range and accuracy;
  • applicable prerequisites described in the test procedures were satisfied;
  • test frequency met TS requirements to demonstrate operability and reliability; 13* the tests were performed in accordance with the test procedures and otherapplicable procedures;* jumpers and lifted leads were controlled and restored where used;
  • test data/results were accurate, complete, and valid;
  • test equipment was removed after testing;
  • where applicable for inservice testing activities, testing was performed inaccordance with the applicable version of ASME Code,Section XI, and reference values were consistent with the system design basis;* where applicable, test results not meeting acceptance criteria were addressedwith an adequate operability evaluation or declared inoperable;* where applicable for safety-related instrument control surveillance tests,reference setting data have been accurately incorporated in the test procedure;* equipment was returned to a position or status required to support theperformance of its safety functions; and* all problems identified during the testing were appropriately documented in thecorrective action program.Key documents used by the inspectors in conducting this inspection are listed in theAttachment to this report.

b. Findings

No findings of significance were identified.

1R23 Temporary Plant Modifications (71111.23)

a. Inspection Scope

The inspectors conducted in-plant observations of the physical changes to theequipment and an in-office review of documentation associated with one temporary modification. This constituted one temporary modification inspection sample. The inspectors reviewed Temporary Modification EC 9802, which was implemented to install a seal on the snubber for the feedwater control valve to the 21 steam generator, CV-31135, as a temporary repair for an oil leak.The inspection activities included a review of design documents, safety screeningdocuments, and the USAR to determine that the temporary modification was consistent with modification documents, drawings, and procedures. The inspectors also reviewed the post-installation test results to confirm that tests were satisfactory and the actual impact of the temporary modification on the permanent system and interfacing systems were adequately verified. Additionally, the inspectors reviewed the corrective action documentation associated with an identified problem with the air supply to the power operated relief valves to verify that the licensee was identifying issues at an appropriate threshold and entering them into their corrective action program in accordance with station corrective action. The key documents reviewed by the inspectors are listed in the Attachment to this report.

b. Findings

No findings of significance were identified.Cornerstone: Emergency Preparedness1EP6Drill Evaluation (71114.06)

a. Inspection Scope

The inspectors observed the licensee perform an emergency preparedness drill onFebruary 6, 2007. This inspection effort completed one emergency planning drill evaluation sample. The inspectors observed activities in the Technical Support Center and OperationsSupport Center and attended the post-drill critique on February 6, 2007. The focus of the inspectors' activities was to note any weaknesses and deficiencies in the drill performance and ensure that the licensee evaluators noted the same weaknesses and deficiencies and entered them into the corrective action program. The inspectors placed emphasis on observations regarding event classification, notifications, protective action recommendations, and site evacuation and accountability activities. Key documents used by the inspectors in conducting this inspection are listed in the Attachment to this report.

b. Findings

No findings of significance were identified.2.RADIATION SAFETYCornerstone: Occupational Radiation Safety2OS1Access Control to Radiologically Significant Areas (71121.01)

.1 Review of Licensee Performance Indicators for the Occupational Exposure Cornerstone

a. Inspection Scope

The inspectors reviewed the licensee's occupational exposure control cornerstoneperformance indicators (PIs) to determine whether or not the conditions surrounding the PIs had been evaluated and to determine if identified problems had been entered into the corrective action program for resolution. This review represented one sample.

b. Findings

No findings of significance were identified.

.2 Plant Walkdowns and Radiation Work Permit Reviews

a. Inspection Scope

The inspectors identified radiologically significant work areas within radiation areas, highradiation areas (HRAs), locked high radiation areas (LHRAs), and airborne areas in the auxiliary and containment buildings. Selected work packages and radiation work permits (RWPs) were reviewed to determine if radiological controls, including surveys, postings, air sampling data and barricades, were acceptable. Work areas included, but were not limited to:*Wooden Door with Metal Door at Spent Resin Tank Replacement;*2R24 Incore Drives;

  • 2R24 Containment Inspections;
  • 2R24 Insulation Removal; and
  • Resin Liner No. 129 to the Shipping Cask Transfer.This review represented one sample.

The inspectors reviewed selected RWPs and associated radiological controls used toaccess these and other radiologically significant areas and evaluated the work control instructions and control barriers that were specified in order to determine if the controls and requirements provided adequate worker protection. The Site Technical Specification requirements for HRAs and locked high radiation areas were used as standards for the necessary barriers. Electronic dosimeter alarm set points for both integrated dose and dose rate were evaluated for conformity with survey indications and plant policy.This review represented one sample.

b. Findings

No findings of significance were identified.

.3 Problem Identification and Resolution

a. Inspection Scope

The inspectors reviewed the licensee's self-assessments, audits, and condition reports related to the access control program to determined if identified problems were entered into the corrective action program for resolution.This review represented one sample.

Corrective action reports related to access controls and high radiation area radiologicalincidents (non-performance indicator occurrences identified by the licensee in HRAs of less than 1Rem/hr) were reviewed. Selected staff members were interviewed and a selected sample of corrective action documents were reviewed to determine if follow-up 16activities were conducted in an effective and timely manner commensurate with theirimportance to safety and risk based on the following:*initial problem identification, characterization, and tracking;*disposition of operability/reportability issues;

  • evaluation of safety significance/risk and priority for resolution;
  • identification of repetitive problems;
  • identification of contributing causes;
  • identification and implementation of effective corrective actions;
  • resolution of Non-Cited Violations (NCV) tracked in the corrective action system; and*implementation/consideration of risk significant operational experience feedback.This review represented one sample.

The inspectors determined if the licensee's self-assessment and audit activitiescompleted for the year that preceded the inspection were identifying and addressing repetitive deficiencies or significant individual deficiencies in problem identification andresolution, as applicable. This review represented one sample.

The inspectors discussed performance indicators with the radiation protection staff andreviewed data from the licensee's corrective action program to determine if there were any performance indicators for the occupational exposure cornerstone that had not been reviewed. There were none to evaluate. This review represented one sample.

b. Findings

No findings of significance were identified.

.4 High Risk Significant, High Dose Rate High Radiation Area, and Very High RadiationArea Controls

a. Inspection Scope

The inspectors reviewed the licensee's performance indicators for high risk, high doserate HRAs, and for very high radiation areas to determine if workers were adequately protected from radiological overexposure. Discussions were held with selected radiation protection management and technicians concerning high dose rate HRA and very high radiation area controls and procedures, including procedural changes that had occurred since the last inspection. This review was completed to determine if procedure modifications had substantially reduced the effectiveness and level of worker protection.

This review represented one sample.The inspectors interviewed radiation protection (RP) supervisors to determine if plantevolutions that could impact radiological conditions were communicated between the RP 17group and other involved groups beforehand in order to allow corresponding timelyactions to properly post and control the radiation hazards. This review represented one

sample.During plant walkdowns, the posting and locking of entrances to high dose rate HRAs,and very high radiation areas were reviewed for adequacy. This review represented one

sample.

b. Findings

One finding of very low safety significance was identified.

Introduction:

A Green finding and associated NCV was identified when an NRCinspector reviewed an issue where a station operator entered without authorization into an LHRA while personnel were moving a high integrity container (HIC) to the radioactive waste barrel yard.Description: On December 4, 2006, Prairie Island station personnel were transferringHIC No. 129 containing radioactive resin from the back of a flat bed trailer into a HIC storage area in the radioactive waste barrel yard. The dose rates on the HIC were 18,000 millirem per hour (mRem/hr) at contact; 8,000 mRem/hr at a distance of one foot; and 3,000 mRem/hr at a distance of one meter. Given these radiological conditions, the HIC transfer work area was posted and controlled in accordance with station procedures and Technical Specification 5.7.2 as a locked high radiation area.

Station procedures and 10 CFR 20.1903 permit certain exceptions to radiological posting requirements for short periods of time so long as specified alternate measures are in place. At Prairie Island the alternate actions for LHRA posting and access control was achieved through the use of LHRA guards at various access points. Locked high radiation area guards were personnel specifically assigned to control access to radiologically significant areas of the plant. At Prairie Island, the specific responsibilitiesof the LHRA guards were defined in station procedure PINGP 1470 and included the requirement that LHRA guards not allow unauthorized or inadvertent access into the LHRA. On December 4, 2006, at approximately 10:30 a.m., a station operator, whileresponding to a high level tank alarm on the radioactive waste liquid processing panel in the radioactive waste facility, entered a LHRA that was controlled by a LHRA guard.

The operator was not on an RWP that permitted access to locked high radiation areas and was not pre-briefed on the radiological conditions specific to the work area being entered nor the potential impact of the transient radiological conditions being created by the HIC transfer activities. The operator was advised by the LHRA guard not to enter the radioactive waste processing area, however, the operator was not specifically informed that the area was being controlled for radiological purposes as a locked high radiation area. Consequently, the operator entered the LHRA because the radiological status of the area was not clearly communicated by the LHRA guard.Analysis: The inspectors determined that the LHRA guard allowed unauthorized entryinto the area contrary to procedural requirements which represents a performance deficiency and a finding as described in IMC 0612, Appendix B, "Issue Screening." The 18issue was more than minor because it was associated with the Program/Processattribute of the Occupational Radiation Safety cornerstone and potentially affected the cornerstone objective to ensure worker health and safety from exposure to radiation.

The finding does not involve the application of traditional enforcement, because it did not result in actual safety consequences or the potential to impact the NRC's regulatory function, and was not the result of willful actions. The finding was evaluated using the SDP in accordance with IMC 0609, Appendix C, for the Occupational Radiation Safety cornerstone. The finding was determined to be of very low safety significance (Green)because it did not involve As-Low-As-Reasonably-Achievable (ALARA) planning, was not associated with an overexposure given the actual radiological conditions in the area, and there were other workers present in the general area of the HIC transfer that could have interceded to minimize any actual radiological exposure. Consequently, there was not a substantial potential for a worker overexposure and the licensee's ability to assess worker dose was not compromised.However, this issue was not entered into the licensee's corrective action program in atimely manner and the evaluation of the issue was not comprehensive or thorough relative to regulatory impact on station technical specifications or 10 CFR Part 20 compliance. Additionally, the licensee's evaluation did not fully develop the cause of the event nor evaluate this event in relationship to previous events concerning the performance and effectiveness of LHRA guards. Specifically, Prairie Island had a similar event involving the performance of LHRA guards controlling access to radiologically significant areas during the Unit 1 April 2006 refueling outage. Had that previous event been properly identified, entered into the licensee's corrective action program, and evaluated adequately and in a timely manner, the December 2006 LHRA event may not have occurred.On the night shift of April 28, 2006, a work crew was in the Unit 1 containment airlock(a posted locked high radiation area) without a RP specialist escort. This earlier event, although known to members of the licensee's staff was not entered into the corrective action program until it was brought to the licensee's attention by the NRC approximately nine months later (IR 01075188; dated February 01, 2007). Consequently, this finding also relates to the cross-cutting area of problem identification and resolution dealing with the corrective action program component intended to ensure issues are promptly identified and thoroughly evaluated to allow timely corrective actions.Licensee corrective actions included revising the process for LHRA guards such that theguard obtains positive verification that all radiological requirements are met prior to authorizing entry to an area and training for Nuclear Plant Service Attendants on Technical Specification requirements, area guarding, and command and control techniques.

Enforcement:

Technical Specification 5.4.1.a. requires the licensee to establish,implement, and maintain procedures recommended by Regulatory Guide 1.33, Revision 2, Appendix A, February 1978. Procedures specified in Regulatory Guide 1.33 include RP procedures for access control to radiological areas, which are provided by licensee procedure PINGP 1470, High Radiation Area/Locked High Radiation Area Entry and Control Briefing Sheet (Revision 5). That procedure states that if an LHRA 19guard is assigned, then that person's only responsibilities are to not allow unauthorizedor inadvertent entries into the LHRA.Contrary to the above, on December 4, 2006, a station operator entered an LHRA thatwas being controlled by an LHRA guard and into the radioactive waste facility without proper authorization. Since the finding is of very low safety significance and had been entered into the corrective action system as CAP 1070811, the associated violation is being treated as an NCV, consistent with Section VI.A of the NRC Enforcement Policy (NCV 05000282/2007002-01; 05000306/2007002-01).2OS2As-Low-As-Reasonably-Achievable (ALARA) Planning and Controls (71121.02)

.1 Inspection Planning

a. Inspection Scope

The inspectors reviewed plant collective outage exposure history, current exposuretrends, and ongoing outage activities in order to assess current performance and exposure challenges. This review included determining the plant's current 3-year rolling average for collective exposure in order to help establish resource allocations and to provide a perspective of significance for any resulting inspection finding assessment. The inspectors reviewed the outage work scheduled during the inspection period andassociated work activity exposure and time/labor estimates for the following five-work activities which resulted in the highest personnel collective exposures or were otherwise activities that were conducted in radiologically significant areas: *Wooden Door with Metal Door at Spent Resin Tank Replacement;*2R24 Incore Drives;

  • 2R24 Containment Inspections;
  • 2R24 Insulation Removal; and
  • Resin Liner No. 129 to the Shipping Cask Transfer.The inspectors determined site specific trends in collective exposures based on planthistorical exposure and source term data. The inspectors reviewed procedures associated with maintaining occupational exposures ALARA and assessed those processes used to estimate and track work activity exposures. These reviews represented three inspection samples.

b. Findings

No findings of significance were identified.

.2 Radiological Work Planning

a. Inspection Scope

The inspectors evaluated the licensee's list of work activities ranked by estimatedexposure that were completed during the outage and reviewed the following work activities of highest exposure significance:*Wooden Door with Metal Door at Spent Resin Tank Replacement;*2R24 Incore Drives;

  • 2R24 Containment Inspections;
  • 2R24 Insulation Removal; and
  • Resin Liner No. 129 to the Shipping Cask Transfer.For the activities listed above, the inspectors reviewed the RWP packages, work orders,exposure estimates, and exposure mitigation requirements in order to verify that the licensee had established radiological engineering controls that were based on sound radiation protection principles in order to achieve occupational exposures that were ALARA. This review also involved determining that the licensee had reasonably grouped the radiological work into work activities, based on historical precedence, industry norms, and/or special circumstances. These reviews represented two inspection samples.

b. Findings

No findings of significance were identified.

.3 Verification of Dose Estimates and Exposure Tracking Systems

a. Inspection Scope

The inspectors reviewed the licensee's assumptions and basis for its collective outageexposure estimate and evaluated the methodology and practices for projecting work activity specific exposures. This review included evaluating both dose rate and time/labor estimates for adequacy compared to historical station specific or industry data.This review represented one inspection sample.

b. Findings

No findings of significance were identified.

.4 Problem Identification and Resolution

a. Inspection Scope

The inspectors reviewed the licensee's self-assessments, audits, and Special Reportsrelated to the ALARA program since the last inspection to determine if the licensee's overall audit program's scope and frequency for all applicable areas under the occupational cornerstone met the requirements of 10 CFR 20.1101(c). The licensee's corrective action program was also reviewed to determine if repetitive deficiencies and/or significant individual deficiencies in problem identification and resolution had been addressed.These reviews represented two inspection samples.

b. Findings

No findings of significance were identified.4.OTHER ACTIVITIES4OA1Performance Indicator Verification (71151)Cornerstone: Barrier Integrity

a. Inspection Scope

The inspectors reviewed the licensee's submittals for three performance indicators forPrairie Island Units 1 and 2, completing six PI verification inspection procedure samples.

The inspectors used PI guidance and definitions contained in National Energy Institute Document 99-02, Revision 4, "Regulatory Assessment Performance Indicator Guideline," to verify the accuracy of the PI data. The inspectors' review included conditions and data from logs, condition reports, and calculations for each PI specified.

The inspectors also reviewed the CAPs listed in the Attachment to this report to verify that the licensee was identifying issues at an appropriate threshold and entering them into their corrective action program in accordance with corrective action procedures.The licensee's reporting of the following PIs were verified:

Unit 1*Unplanned Scrams per 7000 Critical Hours for the 1 st Quarter 2006 through the4th Quarter 2006;*Unplanned Scrams with the Loss of Normal Heat Removal 1 st Quarter 2006through the 4 th Quarter 2006; and*Unplanned Power Changes per 7000 Critical Hours for the 1 st Quarter 2006through the 4 th Quarter 2006.

22Unit 2*Unplanned Scrams per 7000 Critical Hours for the 1 st Quarter 2006 through the4th Quarter 2006;*Unplanned Scrams with the Loss of Normal Heat Removal 1 st Quarter 2006through the 4 th Quarter 2006; and*Unplanned Power Changes per 7000 Critical Hours for the 1 st Quarter 2006through the 4 th Quarter 2006.Key documents used by the inspectors in conducting this inspection are listed in theAttachment to this report.

b. Findings

No findings of significance were identified.4OA2Identification and Resolution of Problems (71152)

.1 Routine Review of Identification and Resolution of Problems

a. Inspection Scope

As discussed in previous sections of this report, the inspectors routinely reviewed issuesduring baseline inspection activities and plant status reviews to verify that they were being entered into the licensee's corrective action program at an appropriate threshold, that adequate attention was given to ensure timely corrective actions, and that adverse trends were identified and addressed. This review did not count as an annual sample.

b. Findings

No findings of significance were identified.

.2 Selected Issue Follow-up Inspection

a. Inspection Scope

The inspectors selected an issue associated with diesel generator D6 generator bearingvibration measurements exceeding the manufacturer's recommended limits for a more in-depth review in accordance with Inspection Procedure 71152, "Identification and Resolution of Problems." This effort completed one in-depth review of the Problem Identification and Resolution inspection sample to review the corrective action aspects associated with this event. The inspectors reviewed the evaluation and corrective actions. The key documents reviewed by the inspectors associated with this inspection are listed in the Attachment to this report.

b. Findings and Observations

No findings of significance were identified. The licensee evaluated the impact of thevibration on the operability of the diesel generator and concluded that D6 was fully 23capable of performing its specified safety functions. The licensee has developed acorrective action plan to address the elevated vibration during the next scheduled maintenance period.4OA3Event Followup (71153)(Closed) Licensee Event Report (LER) 05000306/2006-002-00: Unit 2 Event MonitoringInstrument Inoperable Longer Than Allowed by Technical Specifications.On May 5, 2006, during a refueling outage on Unit 1, neutron flux monitor 1N51 and1N52 displayed erratic indications. Troubleshooting and investigation involved purging moisture from the cables and performing a pressure test. The pressure test was not successful for 1N51 and subsequent inspection of the cables revealed that a cable splice connection sleeve did not include a shim that was required for the gap between the outside diameter of the cable and the inside diameter of the sleeve. During the Unit 2 refueling outage, licensee's staff inspected the cables for the Unit 2neutron flux monitor channels 2N51 and 2N52. The licensee's staff found that the respective cables for 2N51 and 2N52 did not have the required shim in the sleeves for the splice connections. The inspectors reviewed the LER, CAPs, evaluation, and corrective actions, and no findings of significance were identified. The issue was considered minor because none of the minor questions from IMC 0612, Appendix B, dated November 2, 2006, were answered in the affirmative. Specifically, the performance deficiency did not result in a loss of system safety function, and the inspectors did not identify any earlier opportunities for identification of the problem by the licensee. This LER is closed.4OA5Other Activities

.1 (Closed) Unresolved Item (URI) 050000282/2006002-02; 050000306/2006002-02:

Licensee Continuing On-site Tritium Well Sample Results AssessmentThe inspectors reviewed the licensee's progress in investigating the cause of theseasonally elevated tritium levels in the water in a singular on-site monitoring well (P-10). The licensee conducted additional analysis of their on-site water monitoring program including a self-assessment and a hydrological review. Although there was not sufficient data to confirm a link or definitively exclude other potential sources, the licensee determined that the most likely contributor to the fluctuating tritium levels in the (P-10) well samples was radionuclide migration of discharges from the turbine building sump. The turbine building sump was a monitored effluent discharge pathway that, by plant design, may contain small but measurable amounts of tritiated water. The contents of the turbine building sump were routinely analyzed, characterized, and the radiological impact of any discharge to the land lock was evaluated in accordance with the Off-Site Dose Calculation Manual. The licensee continued to monitor and evaluate the analytical results from its on-site well water program relative to their groundwater protection initiative program. Anomalous sample results were assessed for radiological impact and identified findings were reported in the Annual Effluent Report. Based on the licensee's evaluation, the continued onsite well monitoring program was in compliance with the Off-Site Dose Calculation Manual, this item is closed.

244OA6Meeting(s)

.1 Exit MeetingOn April 4, 2007, the resident inspectors presented the inspection results toMr. T. Palmisano and other members of his staff, who acknowledged the finding.

The inspectors asked the licensee whether any of the material examined during the inspection should be considered proprietary. No proprietary information was identified.

.2 Interim Exit MeetingsInterim exits were conducted for:

  • Biennial Operator Requalification Program inspection with Mr. J. Lash, TrainingManager, on January 23, 2007; and *Access control to radiologically significant areas and ALARA program inspectionwith Mr. P. Huffman, Plant Manager, on February 02, 2007, with a followup teleconference to discuss the final outcome of the inspection with Mr. J. Kivi, Compliance Engineer, on March 21, 2007.ATTACHMENT:

SUPPLEMENTAL INFORMATION

KEY POINTS OF CONTACT

Licensee

T. Palmisano, Site Vice President
J. Sorensen, Site Director
P. Huffman, Plant Manager

M.Carlson, Engineering Director

J. Anderson, Radiation Protection Manager
F. Forrest, Operations Manager
J. Lash, Training Manager
S. Northard, Nuclear Safety Assurance Manager
R. Womack, Production Planning Manager
J. Kivi, Regulatory Compliance EngineerNuclear Regulatory Commission
R. Skokowski, Chief, Reactor Projects Branch 3

LIST OF ITEMS OPENED, CLOSED, AND DISCUSSED

Opened05000282/2007002-01NCVFailure to Properly Control Access to a Locked HighRadiation Area

Closed

05000282/2007002-01NCVFailure to Properly Control Access to a Locked HighRadiation Area05000306/2006-002-00LERUnit 2 Event Monitoring Instrument Inoperable LongerThan Allowed by Technical Specifications05000282/2006002-02

05000306/2006002-02URILicensee Continuing On-site Tritium Well Sample

Results Assessment

Discussed

None

2

LIST OF DOCUMENTS REVIEWED

The following is a list of documents reviewed during the inspection.

Inclusion on this list doesnot imply that the NRC inspectors reviewed the documents in their entirety but rather that