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{{#Wiki_filter:May 11, 2021
{{#Wiki_filter:
Mr. Ken Peters
Senior Vice President
  and Chief Nuclear Officer
VISTRA Operating Company, LLC
P.O. Box 1002
Glen Rose, TX 76043
SUBJECT:        COMANCHE PEAK NUCLEAR POWER PLANT, UNITS 1 AND 2 -
                INTEGRATED INSPECTION REPORT 05000445/2021001 AND
                05000446/2021001
Dear Mr. Peters:
On March 31, 2021, the U.S. Nuclear Regulatory Commission (NRC) completed an inspection
at Comanche Peak Nuclear Power Plant, Units 1 and 2. On April 16, 2021, the NRC inspectors
discussed the results of this inspection with Mr. Thomas McCool and other members of your
staff. The results of this inspection are documented in the enclosed report.
One finding of very low safety significance (Green) is documented in this report. This finding did
not involve a violation of NRC requirements.
If you disagree with a finding not associated with a regulatory requirement in this report, you
should provide a response within 30 days of the date of this inspection report, with the basis for
your disagreement, to the U.S. Nuclear Regulatory Commission, ATTN: Document Control
Desk, Washington, DC 20555-0001; with copies to the Regional Administrator, Region IV; and
the NRC Resident Inspector at Comanche Peak Nuclear Power Plant, Units 1 and 2.
 
K. Peters                                        2
This letter, its enclosure, and your response (if any) will be made available for public inspection
and copying at http://www.nrc.gov/reading-rm/adams.html and at the NRC Public Document
Room in accordance with Title 10 of the Code of Federal Regulations 2.390, Public
Inspections, Exemptions, Requests for Withholding.
                                              Sincerely,
                                              Cornelius F.        Digitally signed by
                                                                  Cornelius F. O'Keefe
                                              O'Keefe            Date: 2021.05.11
                                                                  12:38:11 -05'00'
                                              Neil F. O'Keefe, Chief
                                              Reactor Projects Br B
                                              Division of Reactor Projects
Docket Nos. 05000445 and 05000446
License Nos. NPF-87 and NPF-89
Enclosure:
As stated
cc w/ encl: Distribution via LISTSERV
 
 
ML21131A095
                                Non-Sensitive                      Publicly Available
        SUNSI Review
                                Sensitive                          Non-Publicly Available
  OFFICE SRI:DRP/B      RI:DRP/B                TL:DRS/IPAT  BC:DRS/EB1
  NAME    JEllegood JAE NDay NHD                AAgrawal ANA VGaddyvgg
  DATE    05/10/2021    04/28/2021              5/6/2021    05/06/2021
  OFFICE BC:DRS/EB2      ABC:DRS/RCB            BC:DRS/OB    ABC:DNMS/RxIB
  NAME    NTaylor NHT  JRollins JMR            HGepford hjg NGreene / NAG
  DATE    5/6/2021      5/10/2021              5/10/2021    05/06/2021
  OFFICE SPE:DRP/B      BC:DRP/B
  NAME    DProulx DLP  NOKeefe nfo
  DATE    5/10/2021    5/11/21
                                 
                          U.S. NUCLEAR REGULATORY COMMISSION
                                        Inspection Report
Docket Numbers:        05000445 and 05000446
License Numbers:      NPF-87 and NPF-89
Report Numbers:        05000445/2021001 and 05000446/2021001
Enterprise Identifier: I-2021-001-0095
Licensee:              VISTRA Operating Company, LLC
Facility:              Comanche Peak Nuclear Power Plant, Units 1 and 2
Location:              Glen Rose, TX
Inspection Dates:      January 1, 2021 to March 31, 2021
Inspectors:            L. Brookhart, Senior Spent Fuel Storage Inspector
                      N. Day, Resident Inspector
                      J. Drake, Senior Reactor Inspector
                      J. Ellegood, Senior Resident Inspector
                      S. Hedger, Emergency Preparedness Inspector
                      J. Melfi, Project Engineer
Approved By:          Neil F. O'Keefe, Jr., Chief
                      Reactor Projects Br B
                      Division of Reactor Projects
                                                                        Enclosure
 
                                              SUMMARY
The U.S. Nuclear Regulatory Commission (NRC) continued monitoring the licensees
performance by conducting an integrated inspection at Comanche Peak Nuclear Power Plant,
Units 1 and 2, in accordance with the Reactor Oversight Process. The Reactor Oversight
Process is the NRCs program for overseeing the safe operation of commercial nuclear power
reactors. Refer to https://www.nrc.gov/reactors/operating/oversight.html for more information.
                                  List of Findings and Violations
  Failure of Unit 1 Turbine First Stage Pressure Line
  Cornerstone            Significance                                Cross-Cutting    Report
                                                                      Aspect          Section
  Mitigating            Green                                        None (NPP)      71111.12
  Systems                FIN 05000445/2021001-01
                        Open/Closed
  The inspectors identified a finding of very low safety significance, Green, following the failure
  of a weld on the root valve for the main turbine first stage pressure transmitter 1-PT-0505.
  Specifically, the licensee replaced the valve during the fall 2020 refueling outage. The new
  valve was not the same model as the installed valve which resulted in premature failure of a
  weld because the new valve induced harmonic vibration, resulting in an unplanned shutdown
  to make repairs. The licensee failed to properly control inventory in the supply system. As a
  result, the licensee installed a valve in the plant without doing the necessary part evaluations
  needed to verify it was appropriate for the application.
                                    Additional Tracking Items
None.
                                                  2
 
PLANT STATUS
Units 1 began the inspection period at or near 100 percent power. On March 29, 2021, Unit 1
main feedwater pump A tripped. An automatic runback occurred in response to the main
feedwater pump trip which reduced power to about 57 percent. Unit 1 remained at about 57
percent power for the remainder of the inspection period.
Unit 2 operated at or near rated thermal power for the entire inspection period.
INSPECTION SCOPES
Inspections were conducted using the appropriate portions of the inspection procedures (IPs) in
effect at the beginning of the inspection unless otherwise noted. Currently approved IPs with
their attached revision histories are located on the public website at http://www.nrc.gov/reading-
rm/doc-collections/insp-manual/inspection-procedure/index.html. Samples were declared
complete when the IP requirements most appropriate to the inspection activity were met
consistent with Inspection Manual Chapter (IMC) 2515, Light-Water Reactor Inspection
Program - Operations Phase. The inspectors reviewed selected procedures and records,
observed activities, and interviewed personnel to assess licensee performance and compliance
with Commission rules and regulations, license conditions, site procedures, and standards.
Starting on March 20, 2020, in response to the National Emergency declared by the President
of the United States on the public health risks of the Coronavirus Disease 2019 (COVID-19),
resident inspectors were directed to begin telework and to remotely access licensee information
using available technology. During this time, the resident inspectors performed periodic site
visits each week; conducted plant status activities as described in IMC 2515, Appendix D, Plant
Status; observed risk-significant activities; and completed on-site portions of IPs. In addition,
resident and regional baseline inspections were evaluated to determine if all or portions of the
objectives and requirements stated in the IP could be performed remotely. If the inspections
could be performed remotely, they were conducted per the applicable IP. In some cases,
portions of an IP were completed remotely and on-site. The inspections documented below met
the objectives and requirements for completion of the IP.
REACTOR SAFETY
71111.01 - Adverse Weather Protection
Seasonal Extreme Weather Sample (IP Section 03.01) (1 Sample)
    (1)    On February 11, 2021, the inspectors evaluated readiness for seasonal extreme
            weather conditions prior to the onset of cold weather per procedure OWI-912, Cold
            Weather, for the following systems:
            Station Service Water
            Fire Water
            Emergency Diesel Generators
Impending Severe Weather Sample (IP Section 03.02) (1 Sample)
                                                  3
 
    (1)  The inspectors evaluated the adequacy of the overall preparations to protect
          risk-significant systems from impending severe weather for high winds on January 14,
          2021
71111.04 - Equipment Alignment
Partial Walkdown Sample (IP Section 03.01) (2 Samples)
    The inspectors evaluated system configurations during partial walkdowns of the following
    systems/trains:
    (1)  Systems, structures and components in service water and fire water for both units
          that were vulnerable to freezing following extreme cold on February 20, 2021
    (2)  Unit 1, residual heat removal system A following quarterly surveillance on March 11,
          2021
71111.05 - Fire Protection
Fire Area Walkdown and Inspection Sample (IP Section 03.01) (5 Samples)
    The inspectors evaluated the implementation of the fire protection program by conducting a
    walkdown and performing a review to verify program compliance, equipment functionality,
    material condition, and operational readiness of the following fire areas:
    (1)  Flex equipment storage building, area X-FX-2K19, on February 22, 2021
    (2)  Unit 1, main feedwater pumps, area TB, on March 12, 2021
    (3)  Station service water intake structure, area WB, on March 22, 2021
    (4)  Unit 1, safeguards building ventilation, area SK17a, on March 30, 2021
    (5)  Unit 1, main steam isolation and atmosphere relief valve room, area SK17c, on
          March 30, 2021
Fire Brigade Drill Performance Sample (IP Section 03.02) (1 Sample)
    (1)  The inspectors evaluated the onsite fire brigade training and performance during an
          unannounced fire drill on March 18, 2021
71111.06 - Flood Protection Measures
Cable Degradation (IP Section 03.02) (1 Sample)
    The inspectors evaluated cable submergence protection in:
    (1)  Unit 1, station service water cable vault E1B2 on January 28, 2021.
71111.07A - Heat Sink Performance
Annual Review (IP Section 03.01) (1 Sample)
    The inspectors evaluated readiness and performance of:
    (1)  Unit 1, containment spray pump 1-01 and lube oil cooler 1-03
                                                4
 
71111.11Q - Licensed Operator Requalification Program and Licensed Operator Performance
Licensed Operator Performance in the Actual Plant/Main Control Room (IP Section 03.01)
(1 Sample)
    (1)    The inspectors observed and evaluated licensed operator performance in the control
          room during service water restoration on March 26, 2021
Licensed Operator Requalification Training/Examinations (IP Section 03.02) (1 Sample)
    (1)    The inspectors observed and evaluated a simulated complete loss of component
          cooling water on January 27, 2021
71111.12 - Maintenance Effectiveness
Maintenance Effectiveness (IP Section 03.01) (2 Samples)
    The inspectors evaluated the effectiveness of maintenance to ensure the following
    structures, systems, and components (SSCs) remain capable of performing their intended
    function:
    (1)    Unit 1, service water pump fouling on November 18, 2020
    (2)    Failure of Unit 1 PT-0505, turbine first stage pressure transmitter, instrument line on
          November 6, 2020
71111.13 - Maintenance Risk Assessments and Emergent Work Control
Risk Assessment and Management Sample (IP Section 03.01) (6 Samples)
    The inspectors evaluated the accuracy and completeness of risk assessments for the
    following planned and emergent work activities to ensure configuration changes and
    appropriate work controls were addressed:
    (1)    Unit 2, simultaneous scheduling power range nuclear instrument calibrations for N-41
          and N-42 on January 4, 2021
    (2)    Unit 1, unplanned inoperability train B auxiliary feedwater (AFW) pump on January 6,
          2021
    (3)    Recovery of breaker 1A1-1, normal offsite power to nonvital 6.9KVon January 20,
          2021
    (4)    Low temperatures and high grid load during the week of February 15, 2021
    (5)    Extended service water pump 2-02 outage during the week of March 22, 2021
    (6)    Unit 1, repairs to main feed pump A during the week of March 29, 2021
71111.15 - Operability Determinations and Functionality Assessments
Operability Determination or Functionality Assessment (IP Section 03.01) (5 Samples)
                                                  5
 
    The inspectors evaluated the licensee's justifications and actions associated with the
    following operability determinations and functionality assessments:
    (1)    Unit 1, repair of B AFW pump flow transmitter
    (2)    Operability of 2-01 emergency diesel generator with unit trip light illuminated
    (3)    Offsite power with low frequency on February 15, 2021
    (4)    Service water pumps pursuant to Generic Letter 91-13.
    (5)    Circuit breaker 1EB3-3 due to missing overcurrent testing
71111.18 - Plant Modifications
Temporary Modifications and/or Permanent Modifications (IP Section 03.01 and/or 03.02)
(1 Sample)
    The inspectors evaluated the following permanent modification:
    (1)    Unit 1, PT-0505 modification to improve vibration resilience
71111.19 - Post-Maintenance Testing
Post-Maintenance Test Sample (IP Section 03.01) (5 Samples)
    The inspectors evaluated the following post-maintenance test activities to verify system
    operability and functionality:
    (1)    Unit 1, motor driven AFW flow transmitter 1-FT-2457 on
          January 12, 2021
    (2)    Component cooling water pump 1-02 breaker replacement on February 4, 20201.
    (3)    Unit 2, main steam isolation valve 2-03 following pressure gauge root valve leak on
          February 25, 2021
    (4)    Unit 2, replacement of train A accident sequencer optical isolator on March 16, 2021
    (5)    Service water pump 2-02 following replacement on March 27, 2021
71111.22 - Surveillance Testing
The inspectors evaluated the following surveillance tests:
Surveillance Tests (other) (IP Section 03.01) (2 Samples)
    (1)    Unit 2, power range nuclear instrument on January 5, 2021
    (2)    Unit 2, reactor trip breaker B on January 25, 2021
71114.04 - Emergency Action Level and Emergency Plan Changes
Inspection Review (IP Section 02.01-02.03) (1 Sample)
    (1)    The licensee submitted a summary of emergency plan changes (Revision 44) to the
          NRC on November 12, 2020. The inspectors conducted an in-office review of the
          changes from January 4 to 21, 2021. This evaluation does not constitute NRC
          approval
                                                6
 
OTHER ACTIVITIES - BASELINE
71151 - Performance Indicator Verification
The inspectors verified licensee performance indicators submittals listed below:
IE01: Unplanned Scrams per 7000 Critical Hours Sample (IP Section 03.01) (2 Samples)
    (1)    Unit 1 (January 1, 2020, through December 31, 2020)
    (2)    Unit 2 (January 1, 2020, through December 31, 2020)
IE03: Unplanned Power Changes per 7000 Critical Hours Sample (IP Section 03.02) (2
Samples)
    (1)    Unit 1 (January 1, 2020, through December 31, 2020)
    (2)    Unit 2 (January 1, 2020, through December 31, 2020)
IE04: Unplanned Scrams with Complications (USwC) Sample (IP Section 03.03) (2 Samples)
    (1)    Unit 1 (January 1, 2020, through December 31, 2020)
    (2)    Unit 2 (January 1, 2020, through December 31, 2020)
71152 - Problem Identification and Resolution
Annual Follow-up of Selected Issues (IP Section 02.03) (2 Samples)
    The inspectors reviewed the licensees implementation of its corrective action program
    related to the following issues:
    (1)    Lack of engineering rigor on multiple engineering products
    (2)    Unit 1, main feed water pump A cause evaluation and corrective actions described in
          Condition Report 2020-07334
71153 - Followup of Events and Notices of Enforcement Discretion
Event Followup (IP Section 03.01) (1 Sample)
    (1)    The inspectors evaluated the Unit 1 main feedwater pump A trip and licensees
          response on March 29, 2021
    (2)    The inspectors evaluated the response to severe cold weather and grid frequency
          variations during the week of February 13
OTHER ACTIVITIES - TEMPORARY INSTRUCTIONS, INFREQUENT AND ABNORMAL
60855 - Operation of An Independent Spent Fuel Storage Installation (ISFSI)
The inspectors performed a review of the licensees ISFSI activities to verify compliance with
requirements of the Certificate of Compliance 72-1014, License Amendment 7, and the
HI-STORM ISFSI Final Safety Analysis Report (FSAR), Revision 9. The inspectors reviewed
selected procedures, corrective action reports, and records to verify ISFSI operations were
                                                7
 
compliant with the Certificate's Technical Specifications, requirements in the FSAR, and NRC
regulations
Operation Of An ISFSI (1 Sample)
  (1)    The inspectors evaluated the licensees dry cask storage operations, from March 22
          through 26, 2021, during an on-site inspection. The Comanche Peak ISFSI is located
          approximately 2,900 feet southeast of the Unit 1 reactor building within a separate
          protected area. The pad was designed to hold 84 HI-STORM 100S (Version B)
          loaded with the Multi-Purpose Canisters, each with 32 spent fuel assemblies
          (MPC-32). The pad is designed to store the casks in a 6 by 14 array. At the time of
          the routine loading inspection, the Comanche Peak ISFSI pad contained a total of 43
          HI-STORM 100S overpacks. The licensee was in the process of transporting the 44th
          cask to the ISFSI and loading/processing the 45th cask in the spent fuel building
          During the on-site inspection, the inspectors evaluated and observed the following
          activities:
              * Walk-down of the ISFSI haul path
              * Transportation of the 44th cask on the vertical cask transporter from the spent
                  fuel building to the ISFSI
              * Fuel assembly selection and placement into the 45th canister
              * Heavy load lifts using the cask handling crane to remove the transfer cask
                  with the loaded canister from the spent fuel pool to the canister processing
                  area
              * Welding and non-destructive testing of the lid-to-shell weld
              * Processing of the spent nuclear fuel for storage, including bulk water removal,
                  forced helium dehydration, and helium backfill operations
              * Final sealing of the canister, including welding of the vent and port cover
                  plates, non-destructive testing, and helium leak-testing
          The inspectors reviewed and evaluated the following documentation during the
          inspection:
              * Fuel selection evaluations for the canisters loaded since the last NRC ISFSI
                  inspection, the inspectors reviewed the contents of casks 40-45 against the
                  license's Technical Specifications for approved contents
              * Radiation surveys for dose at the owner-controlled boundary to verify
                  compliance with the requirements of 10 CFR 72.104 for calendar years 2019
                  and 2020
              * Selected ISFSI related condition reports (CRs) issued since the last NRC
                  ISFSI inspection (October 2019)
              * Quality assurance (QA) program implementation, including recent QA audits,
                  surveillances, receipt inspection, and quality control activities related to ISFSI
                  operations
              * Compliance to Technical Specifications for operational surveillance activities
                  and FSAR required annual maintenance activities
              * Documentation of annual maintenance activities for the sites cask handling
                  crane and special lifting devices
              * Selected licensee design changes and program changes to the ISFSI
                  performed under the site's 10 CFR 72.48 program
                                                  8
 
                *  Changes made by the licensee in the site's 72.212 Evaluation Report from
                    Revisions 11 to 12
INSPECTION RESULTS
  Failure of Unit 1 Turbine First Stage Pressure Line
  Cornerstone            Significance                              Cross-Cutting      Report
                                                                  Aspect            Section
  Mitigating            Green                                    None (NPP)        71111.12
  Systems                FIN 05000445/2021001-01
                        Open/Closed
  The inspectors identified a finding of very low safety significance (Green) following the failure
  of a weld on the main turbine first stage pressure transmitter root valve 1-MS-0285.
  Specifically, the licensee replaced the valve during the fall 2020 refueling outage. The new
  valve was not the same model as the installed valve which resulted in premature failure of a
  weld because the new valve induced harmonic vibration, resulting in an unplanned shutdown
  to make repairs. The licensee failed to properly control inventory in the supply system. As a
  result, the licensee installed a valve in the plant without doing the necessary part evaluations
  needed to verify it was appropriate for the application.
  Description: The licensee replaced the main turbine first stage pressure transmitter root
  valve 1-MS-0285 during the fall 2020 refueling outage as a preventive maintenance
  activity. Shortly after unit start up, on November 6, 2020, main turbine first stage pressure
  transmitter 1-PT-0505 failed low. A parallel indicator continued to function correctly. A
  non-licensed operator investigated the condition and observed a steam plume from the inlet
  side of the instrument root valve 1-MS-0285. Since the leak could not be isolated, the
  licensee shut the unit down and replaced the valve.
  In order to understand the failure, the licensee contracted for an analysis of the failed weld.
  The lab performing the analysis determined the weld failed as a result of fatigue crack
  initiation. Further analysis by the licensee determined the failure occurred as a result of
  vibration at resonant frequency. This resonance response resulted from installation of a
  valve that weighed 2 pounds more than the previously installed valve, which altered the
  natural frequency of the section of piping.
  The inspectors reviewed the licensee's work order associated with valve replacement as well
  as procurement documents associated with the work. Supply chain documents revealed that
  the replacement valve was transferred to Comanche Peak from coal plant. When it arrived,
  the licensee accepted the valve into their inventory under the Texas Utility part number. At
  the time, Texas Utility was the corporate owner of Comanche Peak and numerous fossil
  plants. The licensee correlated the valve to locations for other steam instrument isolation
  valves; however, the valve was not initially correlated to location 1-MS-0285. An update to a
  logistics database in 1998 correlated the part number to the location for 1-MS-0285. In
  reviewing the procedure in effect in 1990, the inspectors determined that the procedure
  required the site to verify the materiel description matched that in the database for the part. If
  it did not, a new part number was required. In this case, the replacement valve did not match
  any valves with an existing part number; however, the licensee failed to assign the valve a
  new part number.
  PT-0505 provides indication of turbine first stage pressure as well as input to Anticipated
  Transient without Scram Mitigation System Actuation Circuitry (AMSAC) and the P-13
  permissive. The AMSAC input allows AMSAC to arm when power is above 40 percent.
                                                  9
 
Since the instrument failed low, AMSAC would not automatically actuate and operators would
have needed to manually initiate AMSAC if the system was needed. The P-13 permissive is
associated with P-7 permissive which blocks certain trips when at low power.
During review of this issue, the licensee identified the technical cause of the weld failure.
However, the licensee did not pursue the underlying cause that allowed an incorrect valve to
be installed. The inspectors discussed potential performance deficiencies with the licensee
which prompted the licensee to understand how the valve was issued for installation. The
licensee plans to incorporate this event into training for supply chain staff.
Corrective Actions: The licensee documented the condition in their Corrective Action
Program (CAP) as CR-2020-8429 and replaced the valve with the correct valve.
Corrective Action References: CR-2020-8429
Performance Assessment:
Performance Deficiency: The licensee failed to properly control inventory in the supply
system. As a result, the licensee installed a valve in the plant without doing the necessary
part evaluations needed to verify it was appropriate for the application. Consequently, the
natural frequency of a high-pressure steam pressure transmitter piping changed causing
premature failure. Repair of the leak required a plant shutdown.
Screening: The inspectors determined the performance deficiency was more than minor
because it was associated with the Design Control attribute of the Mitigating Systems
cornerstone and adversely affected the cornerstone objective to ensure the availability,
reliability, and capability of systems that respond to initiating events to prevent undesirable
consequences. The inspectors determined that the performance deficiency was more than
minor because it adversely affected the mitigating system cornerstone objective of ensuring
the reliability of systems that respond to initiating events. The performance deficiency had a
substantive impact on the equipment performance attribute because the failure of the weld as
a result of the performance deficiency led to PT-0505 unavailability. This instrument provides
input to the P-13 permissive as well as the AMSAC system.
Significance: The inspectors assessed the significance of the finding using Appendix A, The
Significance Determination Process (SDP) for Findings At-Power. The inspectors reviewed
the finding in using Appendix A of IMC 0609. The inspectors answered no to all of the
questions in Exhibit 2, section A because the affected mitigating systems were only briefly
non-functional; therefore, the finding screened as Green.
Cross-Cutting Aspect: Not Present Performance. No cross cutting aspect was assigned to
this finding because the inspectors determined the finding did not reflect present licensee
performance. Specifically, the part designation error occurred in 1998.
Enforcement: Inspectors did not identify a violation of regulatory requirements associated
with this finding.
Observation: Actions to address weaknesses in engineering rigor                        71152
The inspectors noted several examples in 2019 and 2020 regarding weaknesses in
engineering technical rigor. These examples are documented as samples in reports:
05000445/2019004; 05000446/2019004 (ML20041D968)
05000445/2020002; 05000446/2020002 (ML20217L240)
                                                10
 
  05000445/2020004; 05000446/2020004 (ML21040A051)
  The inspectors searched the corrective action program and identified several examples of
  where the site had attempted to improve engineering technical rigor, however, the inspectors
  concluded that the prior efforts had not been sustainable. The inspectors also reviewed a
  presentation on engineering technical rigor provided to engineering staff. The Inspectors
  noted that the training had not been given in over 10 years. The inspectors concluded that
  training on this frequency would not result in sustainable improvement. Subsequently, the
  inspectors discussed actions in place to improve and sustain engineering technical rigor. The
  licensee informed the inspectors that the site would have biennial training on engineering
  technical rigor. In addition, engineering supervisors provide reinforcement of engineering
  rigor during one on one discussions with engineers and in staff meetings. If the licensee
  maintains initiatives to improve engineering rigor, the inspectors expect to see improvement
  in engineering products.
  Observation: Licensee Response to Frigid Weather                                      71153
During the week of February 14, 2021, Comanche Peak experienced frigid weather
conditions for multiple days. Prior to the onset of the cold weather, the licensee
implemented their abnormal procedure to prepare for cold weather with supplemental
actions based on operating experience. The inspectors performed walkdowns of licensee
actions using inspection procedure 71111.01. Following the onset of cold weather, the site
experienced a grid frequency drop on February 15, 2021. As part of the response, as
specified in ABN-601 Response to a 138/345 KV System Malfunction, the licensee started
train A emergency diesel generators in both units and transferred the train A emergency
busses to the diesel. Concurrently, the shift manager contacted the grid operator and
requested the grid operator recover grid frequency to greater than 59.9 Hz. The grid
operator reduced grid load and operators restored the plant to a normal electrical
configuration. The inspectors verified the licensee responded in accordance with approved
procedures by discussion, log reviews, and computer trend reviews. The licensee
maintained the plant in a stable condition with limited work activities for the rest of the
week. The inspectors continued to monitor plant parameters and activities using
procedures 71111.13 and 71111.15. After the cold weather subsided, on February 20,
2021, the inspectors used inspection procedure 71111.04 to inspect the condition of
systems and components susceptible to freezing. The inspectors concluded site personnel
maintained the plant in a safe condition and the cold weather did not cause significant
damage to the plant.
EXIT MEETINGS AND DEBRIEFS
The inspectors verified no proprietary information was retained or documented in this report.
    *  On January 21, 2021, the inspectors presented the Emergency Plan Revision In-Office
        Review Results inspection results to Mr. Patrick Allen, Manager, Emergency
        Preparedness and other members of the licensee staff.
    *  On March 25, 2021, the inspectors presented the routine ISFSI inspection results to
        Mr. Thomas McCool, Site Vice President, and other members of the licensee staff.
    *  On April 16, 2021, the inspectors presented the integrated inspection results to
        Mr. Thomas McCool and other members of the licensee staff.
                                                11
 
DOCUMENTS REVIEWED
Inspection Type              Designation  Description or Title                                    Revision or
Procedure                                                                                          Date
60855      Corrective Action CR-YYYY-NNNN  2019-009399, 2020-001626, 2020-008755, 2021-001243,
            Documents        TR-YYYY-NNNN  TR-2019-008506, TR-2019-009009, TR-2020-000102,
                                            TR-2020-005224
60855      Engineering      EVAL-2019-009 Nuclear Oversight Core Performance Engineering and Fuel 03/11/2020
            Evaluations                    Management QA Audit
60855      Engineering      NUC 212 Cask  Cask Acceptability Report and Comprehensive Assembly    09/05/2019
            Evaluations      40            Specifications Supplement
60855      Engineering      NUC-212 Cask  Cask Acceptability Report and Comprehensive Assembly    09/05/2019
            Evaluations      41            Specifications Supplement
60855      Engineering      NUC-212 Cask  Cask Acceptability Report and Comprehensive Assembly    09/05/2019
            Evaluations      42            Specifications Supplement
60855      Engineering      NUC-212 Cask  Cask Acceptability Report and Comprehensive Assembly    02/24/2021
            Evaluations      43            Specifications Supplement
60855      Engineering      NUC-212 Cask  Cask Acceptability Report and Comprehensive Assembly    02/24/2021
            Evaluations      44            Specifications Supplement
60855      Engineering      NUC-212 Cask  Cask Acceptability Report and Comprehensive Assembly    02/24/2021
            Evaluations      45            Specifications Supplement
60855      Miscellaneous    72.212 Report CPNPP 10CFR72.212 Evaluation Report                    12
60855      Procedures        DCS-201      Transporting Loaded and Unloaded HI-STORM              9
60855      Procedures        DCS-202      MPC Preparation for Loading                            9
60855      Procedures        DCS-203      MPC Handling and Fuel Loading Operations                12
60855      Procedures        DCS-204      MPC Closure Operations (Sealing, Drying, Backfilling)  13
60855      Procedures        DCS-205      Stack-up and Transfer of Loaded MPC                    10
60855      Procedures        OPT-102A-1    Operations Shiftly Routine Tests                        15
71111.01  Work Orders                    5939919
71111.04  Procedures        SOP-102A      Residual Heat Removal System                            22
71111.04  Work Orders                    5820443
71111.05  Fire Plans        FPI-108A      Fire Preplan for UNIT 1 SAFEGUARDS BUILDING MAIN        4
                                            STEAM PENETRATION AREA 880'-6"
71111.05  Fire Plans        FPI-2001      Fire Preplan for FLEX STORAGE BUILDING X-FX-2K19        1
71111.05  Fire Plans        FPI-302A      Fire Preplan for UNIT 1 & 2 TURBINE BUILDING            8
                                            ELEVATION 803'-0"
                                                      12
 
Inspection Type              Designation    Description or Title                                          Revision or
Procedure                                                                                                  Date
71111.05  Fire Plans        FPI-701        Fire Preplan for SERVICE WATER INTAKE STRUCTURE                4
                                            ELEV. 796'-0" & 810'-6"
71111.07A NDE Reports                        Containment Spray Pump 1-01 and 1-03 Visual Inspection        01/20/2021
                                            Report
71111.12  Corrective Action CR-YYYY-NNNN    2020-7695, 2020-8429
          Documents
71111.12  Miscellaneous                    Service water system health report                            08/25/2020
71111.12  Miscellaneous                    Maintenance Rule Database for Main Steam
71111.12  Miscellaneous                    Maintenance Rule Database for Unit 1 Service Water
71111.12  Miscellaneous    6S832645        Material Transfer Form                                        05/01/1990
71111.12  Miscellaneous    MDIR-98-000314-                                                                03/13/1998
                            00-00
71111.12  Procedures        MMO-6.09        TSN Assignment and Transfer of Warehouse Material.            0
71111.13  Procedures        STI-600.01,    Protecting Plant Equipment and Sensitive Equipment            3
                                            Controls
71111.15  Corrective Action CR-YYYY-NNNN    2021-001393, 2021-1224, 2021-553
          Documents
71111.15  Miscellaneous    PQE 208        Rosemont Pressure Transmitter Plant Qualification              12/23/2018
                                            Evaluation
71111.18  Engineering      FDA-2017-      Modify 1-PT-0505                                              2
          Changes          000020-01-01
71111.19  Procedures        OPT-205B        Containment Spray System Post Test for WO 5813767 and          18
                                            5813740
71111.19  Work Orders                      5405494, 595445
71111.19  Work Orders                      5958368
71111.22  Work Orders                      5790214
71114.04  Miscellaneous                    Comanche Peak Nuclear Power Plant Emergency Plan,              43
                                            Units 1 and 2
71114.04  Miscellaneous    AI-TR-2020-    Use of Terms "Onsite," "Offsite," "Site," "Site Boundary," and 09/16/2020
                            000756-13      "Exclusion Area" in the Emergency Plan
71114.04  Miscellaneous    CP-20200627,    Comanche Peak Nuclear Power Plant (CPNPP), Docket              11/12/2020
                            TXX-20093      Nos. 50-445, 50-446; Transmittal of Revised Emergency
                                            Plan (Revision 44)
71114.04  Miscellaneous    EV-TR-2018-    Remove Letter of Agreement References from Comanche            08/18/2020
                                                      13
 
Inspection Type              Designation  Description or Title                                  Revision or
Procedure                                                                                        Date
                            005896-5    Peak Emergency Plan Appendix H
71114.04  Procedures        EPP-123      10 CFR 50.54(q) Screening and Evaluation of Changes to 2
                                          Emergency Plan Documentation
71152      Corrective Action CR-YYYY-NNNN 2018-1550, 2018-2038, 2020-008417
          Documents
71152      Corrective Action TR-YYYY-NNNN 2018-2038 ,2018-5898, 2020-5057, 2021-000414
          Documents
                                                    14
}}
}}

Revision as of 12:58, 8 September 2021

CP2021001-RP-JE, Comanche Peak Nuclear Power Plant, Units 1 and 2 - Integrated Inspection Report 05000445/2021001 and 05000446/2021001
ML21131A095
Person / Time
Site: Comanche Peak  Luminant icon.png
Issue date: 05/11/2021
From: O'Keefe N
NRC/RGN-IV/DRP
To: Peters K
Vistra Operating Co. (VistraOpCo)
References
IR 2021001
Download: ML21131A095 (17)


See also: IR 05000445/2021001

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