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                                  ENCLOSURE 1
*
                              INTERIM SALP REPORT
ENCLOSURE 1
                    U. S. NUCLEAR REGULATORY COMMISSION
INTERIM SALP REPORT
                  OFFICE OF NUCLEAR REACTOR REGULATION
U. S. NUCLEAR REGULATORY COMMISSION
              SYSTEMATIC ASSESSMENT OF LICENSEE PERFORMANCE
OFFICE OF NUCLEAR REACTOR REGULATION
                                                                        ,
SYSTEMATIC ASSESSMENT OF LICENSEE PERFORMANCE
                        NRC INSPECTION REPORT NUMBER                   i
,
                                                                        !
NRC INSPECTION REPORT NUMBER
                        50-327/89-01 AND 50-328/89-01
i
                J
!
                    TENNESSEE VALLEY AUTHORITY (TVA)
50-327/89-01 AND 50-328/89-01
                  SEQUOYAH NUCLEAR PLANT, UNITS 1 AND 2
J
                    FEBRUARY 4, 1988 - FEBRUARY 3, 1989
TENNESSEE VALLEY AUTHORITY (TVA)
                                                        .
SEQUOYAH NUCLEAR PLANT, UNITS 1 AND 2
                                                                          i
FEBRUARY 4, 1988 - FEBRUARY 3, 1989
                                                                          ;
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TABLE OF CONTENTS
PAGE
I.
INTRODUCTION..................................................
-1
A.
Licensee Activities.....................................
2
B.
Direct inspection and Review Activities.................
5
i'
II.
SUMMARY OF RESULTS...........................................
7
A.
Basis Period Summary....................................
7
!
B.
Assessment Period Summary..............................
17
C.
0verview...............................................
18
Ill. CRITERIA....................................................
19
IV.
PERFORMANCE ANALYSIS........................................
20
.
i
A.
Plant 0perations.......................................
20
.
B.
Radiological
Controls..................................
27
C.
Maintenance / Surveillance...............................
30
D.
Emergency Preparedness.................................
39
E.
Security...............................................
40
F.
Engi.neering/ Technical. Support..........................
42
G.-
Safety Assessment /Quali ty Verification. . . . . . . . . . . . . . . . . ., 48
V.
SUPPORTING DATA AND SUMMARIES...............................
54
i
A.
Investigation Review...................................
54
B.
Escalated Enforcement Action...........................
55
C.
Management Conferences.................................
55
D.
Confirmation of Action Letters.........................
56
E.
Review of Licensee Event Reports.......................
57
F.
Licensing Activities...................................
57
G.
Enforcement Activity...................................
63
H.
Re a c t o r T r i p s . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . .
6 3
I.
E f fl u e nt R el e a s e S umm a ry . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . .
64
J.
Acronyms...............................................
64
I
.
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                                                                TABLE OF CONTENTS
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                                                                                                                                      PAGE
l
                  I.  INTRODUCTION..................................................                                                      -1
]
                      A.  Licensee Activities.....................................                                                        2
                      B.  Direct inspection and Review Activities.................                                                        5
                                                                                                                                              i
                                                                                                                                              '
                  II.  SUMMARY OF RESULTS...........................................                                                        7
                      A.  Basis Period        Summary.................................... 7
!                      B.  Assessment Period Summary.............................. 17
                      C.  0verview...............................................                                                      18
                  Ill. CRITERIA....................................................                                                      19
                  IV.  PERFORMANCE ANALYSIS........................................                                                      20  .
                                                                                                                                              i
                      A.  Plant 0perations.......................................                                                    .
                                                                                                                                          20
                      B.  Radiological Controls..................................                                                      27
                      C.  Maintenance / Surveillance...............................                                                    30
                      D.  Emergency Preparedness.................................                                                      39
                      E.  Security...............................................                                                      40
                        F.  Engi.neering/ Technical. Support..........................                                                    42
                      G.-  Safety Assessment /Quali ty Verification. . . . . . . . . . . . . . . . . ., 48
                  V.  SUPPORTING DATA AND SUMMARIES...............................                                                      54
                                                                                                                                              i
                      A.    Investigation        Review...................................                                              54
                        B.  Escalated Enforcement Action...........................                                                      55
                      C.  Management Conferences.................................                                                      55
                        D.  Confirmation of Action Letters.........................                                                      56
                        E.  Review of Licensee Event Reports.......................                                                      57
                        F. Licensing Activities...................................                                                      57
                      G.    Enforcement Activity...................................                                                      63
                        H.  Re a c t o r T r i p s . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . .  63
                        I.  E f fl u e nt R el e a s e S umm a ry . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . .          64
                        J.  Acronyms...............................................                                                      64
                                                                                                                                                I
                                                                                                                            .
                                                                                                                                                l
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                                                                                                                                                ]


                                                                                              _ _ _ _ _ - _ _ _ _ _ -
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                    I. INTRODUCTION
I.
                        The Systematic Assessment of Licensee Performance (SALP) program is an
INTRODUCTION
                        integrated NRC staff effort to collect available observations and data on
The Systematic Assessment of Licensee Performance (SALP) program is an
                        a periodic basis and to evaluate licensee performance on the basis of this
integrated NRC staff effort to collect available observations and data on
                        information. The program is supplemental to normal regulatory prococses
a periodic basis and to evaluate licensee performance on the basis of this
                        used to ensure compliance with Nuclear Regulatory Commission rules and
information.
                        regulations. It is intended to be sufficiently diagnostic to provide a
The program is supplemental to normal regulatory prococses
                        rational basis for allocating Nuclear Regulatory Commission (NRC)
used to ensure compliance with Nuclear Regulatory Commission rules and
                        resources and to provide meaningful feedback to the licensee's management
regulations.
                        regarding the NRC's assessment of their facility's performance in each
It is intended to be sufficiently diagnostic to provide a
                        functional area.                                                                               l
rational basis for allocating Nuclear Regulatory Commission (NRC)
                                                                                                                      )
resources and to provide meaningful feedback to the licensee's management
                        The last SALP appraisal period for Sequoyah was for the period                                 l
regarding the NRC's assessment of their facility's performance in each
                        March 1,1984 through May 31, 1985 with the SALP report being issued on
functional area.
                        September 17, 1985. In August 1985, both units were shutdown for Environ-                     ;
l
                        mental Qualification (EQ) verification. In the September 17, 1985 letter                       j
)
                        transmitting the TVA SALP reports, the NRC communicated that significant
The last SALP appraisal period for Sequoyah was for the period
                        programmatic and management deficiencies existed in TVA's nuclear program
l
                        and pursuant to 10 CFR 50.54(f), TVA was requested to address these de-
March 1,1984 through May 31, 1985 with the SALP report being issued on
                        ficiencies prior to the s'tartup of any nuclear unit.       TVA responded by
September 17, 1985.
                        issuing and implementing the Corporate and Sequoyah Nuclear Performance
In August 1985, both units were shutdown for Environ-
                        Plans. NRC evaluation of the performance plan implementation is docu-
;
                        mented in NUREG-1232, Volumes 1 and 2, respectively, and NRC inspection
mental Qualification (EQ) verification.
                        reports.     Furtier SALP review was deferred pending restart of Unit 2. By
In the September 17, 1985 letter
                        letter dated May 26, 1988, TVA was notified that the normal SALP evalua-
j
                        tion process had recommenced as of February 4,1988.
transmitting the TVA SALP reports, the NRC communicated that significant
                        An NRC SALP Board, composed of the staff member s listed below, met on
programmatic and management deficiencies existed in TVA's nuclear program
                        flarch 28, 1989, to review the observations and data on performance, and
and pursuant to 10 CFR 50.54(f), TVA was requested to address these de-
                        to assess licensee performance in accordance with Chapter NRC-0516,
ficiencies prior to the s'tartup of any nuclear unit.
                        " Systematic Assessment of Licensee Performance." The guidance and evalo-
TVA responded by
                        ation criteria are summarized in Section III of this report.       The Board's
issuing and implementing the Corporate and Sequoyah Nuclear Performance
                        findings and recommendations were forwarded to the Associate Director for
Plans.
                        Special Projects, Office of Nuclear Reactor Regulation, for approval and
NRC evaluation of the performance plan implementation is docu-
                        issuance.
mented in NUREG-1232, Volumes 1 and 2, respectively, and NRC inspection
                        This report is the NRC's assessment of the licensce's safety performance
reports.
                        at Sequoyah for the period February 4,1988 through February 3,1989.
Furtier SALP review was deferred pending restart of Unit 2.
                        The SALP Board for Sequoyah was composed of:
By
                              B. D. Liaw, Director, TVA Projects Division (TVAPD), Office of
letter dated May 26, 1988, TVA was notified that the normal SALP evalua-
                                  fluclear Reactor Regulation (NRR) (Chairman)
tion process had recommenced as of February 4,1988.
                              L. J. Watson, Acting Assistant Director for Inspection Programs,
An NRC SALP Board, composed of the staff member s listed below, met on
                                  TVAPD, NRR
flarch 28, 1989, to review the observations and data on performance, and
                              S. C. Black, Assistant Director for Projects, TVAPD, flRR
to assess licensee performance in accordance with Chapter NRC-0516,
                              R. C. Pierson, Assistant Director for Technical Programs, TVAPD, NRR
" Systematic Assessment of Licensee Performance." The guidance and evalo-
                              D. M. Collins, Chief, Radiological Protection and Emergency
ation criteria are summarized in Section III of this report.
                                  Preparedness Branch, Region II (RII)
The Board's
                              A. F. Gibson, Director, Division of Reactor Safety, RII
findings and recommendations were forwarded to the Associate Director for
                              J. N. Donohew, Senior Project Manager, TVAPD, NRR
Special Projects, Office of Nuclear Reactor Regulation, for approval and
                              K. M. Jenison, Senior Resident Inspector, TVAPD, NRR
issuance.
_     _ - - _ _ - _
This report is the NRC's assessment of the licensce's safety performance
at Sequoyah for the period February 4,1988 through February 3,1989.
The SALP Board for Sequoyah was composed of:
B. D. Liaw, Director, TVA Projects Division (TVAPD), Office of
fluclear Reactor Regulation (NRR) (Chairman)
L. J. Watson, Acting Assistant Director for Inspection Programs,
TVAPD, NRR
S. C. Black, Assistant Director for Projects, TVAPD, flRR
R. C. Pierson, Assistant Director for Technical Programs, TVAPD, NRR
D. M. Collins, Chief, Radiological Protection and Emergency
Preparedness Branch, Region II (RII)
A. F. Gibson, Director, Division of Reactor Safety, RII
J. N. Donohew, Senior Project Manager, TVAPD, NRR
K. M. Jenison, Senior Resident Inspector, TVAPD, NRR
_
_ - - _ _ - _


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        The following staff also attended the Sequoyah SALP Board meeting:                                                 ;
The following staff also attended the Sequoyah SALP Board meeting:
            J. Brady, TVF D, NRR
;
J. Brady, TVF D, NRR
P. Harmon, TVAPD, NRR
,
,
            P. Harmon, TVAPD, NRR
G. Hubbard, TVAPD, NRP,
            G. Hubbard, TVAPD, NRP,
S. Weiss, TVAPD, NRR
            S. Weiss, TVAPD, NRR
B. Zalcman, Technical Assistant, NRR
            B. Zalcman, Technical Assistant, NRR
E. Goodwin, TVAPD, NRR
            E. Goodwin, TVAPD, NRR
B. Desai, TVAPD, NRR
            B. Desai, TVAPD, NRR
K. Landis, RII
            K. Landis, RII
R. Borchardt, RII Coordinator, ED0
            R. Borchardt, RII Coordinator, ED0
T. Rotella, TVAPD, NRR
            T. Rotella, TVAPD, NRR
A.
        A.   Licensee Activities
Licensee Activities
            Both units began the assessment period in shutdown from an extended
Both units began the assessment period in shutdown from an extended
            outage that began in August 1985. TVA agreed, in 1985, not to
outage that began in August 1985.
            restart the units without receiving NRC approval.
TVA agreed, in 1985, not to
            On February 4,1988, Unit 2 received NRC permission to enter Modes 4                                           I
restart the units without receiving NRC approval.
            and 3 (hot shutdown and hot standby) and began the heatup process.
On February 4,1988, Unit 2 received NRC permission to enter Modes 4
            The plant was heated up using reactor coolant pump heat and entered                                           l
I
            Mode 4 on February 6,1988. While in Mode 4, approximately nine                                               i
and 3 (hot shutdown and hot standby) and began the heatup process.
            personnel errors occurred which included inadvertent Main Steam
The plant was heated up using reactor coolant pump heat and entered
            Isolation Valve (MSIV) closures and feedwater isolations, generation
l
            of a reactor trip signal, and a loss of Volume Control Tank (VCT)
Mode 4 on February 6,1988.
            level. None of the events resulting from those personnel errors
While in Mode 4, approximately nine
            represented significant safety concerns of their own accord and
i
            collectively appeared to be typical of what one would expect of a
personnel errors occurred which included inadvertent Main Steam
            near term operating plant going through the same evolution.
Isolation Valve (MSIV) closures and feedwater isolations, generation
            On February 27,1988, Unit 2 entered Mode 3. While in Mode 3, a
of a reactor trip signal, and a loss of Volume Control Tank (VCT)
            number of events occurred including inadvertent closure of all four
level.
            MSIVs, exceeding Technical Specification (TS) surveillance limits for
None of the events resulting from those personnel errors
            Reactor Coolant System (RCS) leakage, exceeding RCS cold leg accumu-
represented significant safety concerns of their own accord and
              lator boron concentration, and two events involving auxilicry
collectively appeared to be typical of what one would expect of a
              feedwater pump operability and charging pump operability of which the
near term operating plant going through the same evolution.
              later involved escalated enforcement. The majority of these events
On February 27,1988, Unit 2 entered Mode 3.
            were personnel related and were responded to by the licensee in an
While in Mode 3, a
                                                                                                                          l
number of events occurred including inadvertent closure of all four
            adequate manner.
MSIVs, exceeding Technical Specification (TS) surveillance limits for
            On March 22, 1988, the NRC Commissioners voted to allow Unit 2 to
Reactor Coolant System (RCS) leakage, exceeding RCS cold leg accumu-
              restart. On March 30, the NRC approved entry into Mode 2 (Startup).
lator boron concentration, and two events involving auxilicry
            On March s1, prior to actually beginning dilution, the licensee
feedwater pump operability and charging pump operability of which the
              determined that modifications would be required on one of the three
later involved escalated enforcement.
              pressurizer safety valve loop seals, and the restart was delayed.
The majority of these events
              During resolution of problems with pressurizer loop seals, a tube
were personnel related and were responded to by the licensee in an
              leak was identified in the #3 steam generator. On April 7, Unit 2
l
              began a cooldown to Mode 5 (cold shoutdown) to repair the steam
adequate manner.
              generator tube leak and complete pressurizer loop seal modifications.
On March 22, 1988, the NRC Commissioners voted to allow Unit 2 to
                                                                                                                      .
restart. On March 30, the NRC approved entry into Mode 2 (Startup).
                                                                        - - . _ _ - _ _ _ . _ _ _ _ _ _ _ _ _ . _ _ _   _
On March s1, prior to actually beginning dilution, the licensee
determined that modifications would be required on one of the three
pressurizer safety valve loop seals, and the restart was delayed.
During resolution of problems with pressurizer loop seals, a tube
leak was identified in the #3 steam generator.
On April 7, Unit 2
began a cooldown to Mode 5 (cold shoutdown) to repair the steam
generator tube leak and complete pressurizer loop seal modifications.
.
- - . _ _ - _ _ _ . _ _ _ _ _ _ _ _ _ . _ _ _
_


  .                                                                                               .__
.
                                                                                                        . _ _ _ _ _
.__
[ni ,.             .
. _ _ _ _ _
[ni
,.
.
l
l
    ..
..
    .-                                                                 3
3
                                                                                        ,
.-
                                      On May' 7', Unit 2 began the heatup process again and entered Mode. 4.
,
                                      On May 11, Unit 2 entered Mode 3 and on May 12, Unit 2 entered Mode 2.
On May' 7', Unit 2 began the heatup process again and entered Mode. 4.
                                      Control rods were withdrawn and dilution to criticality Began. On
On May 11, Unit 2 entered Mode 3 and on May 12, Unit 2 entered Mode 2.
                                      May 13, the reactor achieved criticality, entered Mode 1 (power
Control rods were withdrawn and dilution to criticality Began.
                                      operation), and the generator was synchronized with the grid.           On May
On
                                        15, the NRC granted permission to allow operation above 30% power and
May 13, the reactor achieved criticality, entered Mode 1 (power
                                              .
operation), and the generator was synchronized with the grid.
                                      power escalation was resumed. During the power escalation process
On May
                                      several minor events occurred which included the discovery of an
15, the NRC granted permission to allow operation above 30% power and
                                      unqualified splice in the circuitry for one of the steam generator
.
                                      water level indicators.
power escalation was resumed.
                                      On May 19, Uni 2 tripped from 73% power due to steam flow / feed flow
During the power escalation process
                                      mismatch coincident with low-low steam generator level. This situa-
several minor events occurred which included the discovery of an
                                        tion occurred due to maintenance being performed concurrently cn two
unqualified splice in the circuitry for one of the steam generator
                                        pieces of equipment which together could cause a reactor trip (one
water level indicators.
                                      channel of steam generator level indication to replace the
On May 19, Uni
                                        unqualified splice and the #3 heater drain tank level controller
2 tripped from 73% power due to steam flow / feed flow
                                      which resulted in plant oscillations). On May 20, efter corrective
mismatch coincident with low-low steam generator level.
                                        actions for the trip were completed, NRC permission was given to
This situa-
                                        restart Unit 2.
tion occurred due to maintenance being performed concurrently cn two
                                      On May 21,' Unit 2 achieved criticality. entered Mode 1, and was
pieces of equipment which together could cause a reactor trip (one
                                        synchronized with the grid.                                                     .
channel of steam generator level indication to replace the
                                                                                                                        ;
unqualified splice and the #3 heater drain tank level controller
                                        On May 23, Unit 2 tripped from 70% power on low fbs in RCS Loop #4.
which resulted in plant oscillations).
                                      This occurred due to a personnel error while performing a surveil-
On May 20, efter corrective
                                        lance instruction on the loop #4 flow transmitters.   Or, May 24, Unit
actions for the trip were completed, NRC permission was given to
                                        2 achieved criticality, synchronized with the grid and began power             ;
restart Unit 2.
                                        escalation.
On May 21,' Unit 2 achieved criticality. entered Mode 1, and was
                                                                                                                        1
synchronized with the grid.
                                        On May 24, while Unit I was in partial drain to plug steam generator
.
                                        tubes, a loss of decay heat removal occurred due to an cperatcr error       ,
;
                                        in positioning valves while changing the residual heat removal (RHR)
On May 23, Unit 2 tripped from 70% power on low fbs in RCS Loop #4.
                                        system alignment.
This occurred due to a personnel error while performing a surveil-
                                        On May 29, 1988, Unit-2 achieved 100% reactor power.
lance instruction on the loop #4 flow transmitters.
                                        On June 6,1988, Unit 2 tripped from 98% power on stean flow / feed
Or, May 24, Unit
                                        flow mismatch coincident with low level in #4 steam generator. The             .
2 achieved criticality, synchronized with the grid and began power
                                          trip occurred while performing a surveillance on the feedwater                 l
;
                                          regulating valves and resulted because a diode was missing in the
escalation.
                                        block circuit.
1
                                        On June 8,1988, Unit 2 tripped from T2% power on low-low level in #2
On May 24, while Unit I was in partial drain to plug steam generator
                                          steam generator. The trip was caused by operator error when placing
tubes, a loss of decay heat removal occurred due to an cperatcr error
                                          the feed pump contro'.ler in the automatic position which resulted in         i
,
                                          steam generator level oscillations.
in positioning valves while changing the residual heat removal (RHR)
                                        On June 9, 1988, Unit 2 tripped from 20% power on low-low level in 72
system alignment.
                                          steam generator. The trip was caused by transients in feed flow and
On May 29, 1988, Unit-2 achieved 100% reactor power.
                                          steam generator level which were initiated by feedwater heater
On June 6,1988, Unit 2 tripped from 98% power on stean flow / feed
                                          isolations.
flow mismatch coincident with low level in #4 steam generator. The
                                                                                                                        !
.
                                                                                                                        1
trip occurred while performing a surveillance on the feedwater
        _ . _ _ _ _ _ _ _ - . _ _ - - _ - _
l
regulating valves and resulted because a diode was missing in the
block circuit.
On June 8,1988, Unit 2 tripped from T2% power on low-low level in #2
steam generator.
The trip was caused by operator error when placing
the feed pump contro'.ler in the automatic position which resulted in
i
steam generator level oscillations.
On June 9, 1988, Unit 2 tripped from 20% power on low-low level in 72
steam generator.
The trip was caused by transients in feed flow and
steam generator level which were initiated by feedwater heater
isolations.
!
1
_ . _ _ _ _ _ _ _ - . _ _ - -
_ - _


                  _ _ __ _ _ _ . _
_ _ __ _ _ _ . _
. e.
.-
.-
      ,
,
                            . e.
M'
,.   M'
,.
!
!
  -.
-.
                                                                                        4
4
                                                          'On June 13, 1988, TVA mec with the NRC staff to discuss the root
'On June 13, 1988, TVA mec with the NRC staff to discuss the root
                                                          causes _ for the five reactor trips which had occurred since Unit 2
causes _ for the five reactor trips which had occurred since Unit 2
                                                          restarted on May 18, 1988. Corrective actions identified included
restarted on May 18, 1988.
l                                                         reducing the number of outstanding secondary plant work requests
Corrective actions identified included
                                                          which could contribute to balance of plant induced reactor trips.
l
                                                          On June.19, 1988, the NRC granted permission t'o restart Unit 2. On
reducing the number of outstanding secondary plant work requests
                                                          June 30,1988, Unit 2 reached 70% reactor power (holding for core
which could contribute to balance of plant induced reactor trips.
                                                          life extension).
On June.19, 1988, the NRC granted permission t'o restart Unit 2.
                                                          On September 27, 1988, the NRC granted permission ~for Unit I to enter
On
                                                          Mode 4.   While in Mode 4, several unanticipated reactor trip signals
June 30,1988, Unit 2 reached 70% reactor power (holding for core
                                                          were gener M due to personnel         errors while performing
life extension).
                                                          surveillance.
On September 27, 1988, the NRC granted permission ~for Unit I to enter
                                                          On October 20, 1983, Unit 1 entered Mode 3.   While in Mode 3, the UHI
Mode 4.
                                                          membrane was ruptared while putting the system in service due to.
While in Mode 4, several unanticipated reactor trip signals
                                                          improperly labeleo valves.     Equipment problems such as steam
were gener M due to personnel
                                                          generator safety valve at leakage, pressurizer safety valve seat
errors while performing
                                                        , leakage, reactor vessel inner seal leakage, and steam dump packing
surveillance.
                                                            leakage were encountered and properly resolved.
On October 20, 1983, Unit 1 entered Mode 3.
                                                          On ' November. 6,1988, Unit 1 entered Mode 2 and went critical .   On
While in Mode 3, the UHI
                                                          November 10, 1988, Unit 1 entered Mode 1, the generator was
membrane was ruptared while putting the system in service due to.
                                                          synchronized with the grid, and power escalation began. Several
improperly labeleo valves.
                                                          personnel errors related to equipment surveillance caused ESF
Equipment problems such as steam
                                                          actuations while in Modes 2 and 1.
generator safety valve at leakage, pressurizer safety valve seat
                                                          On November 18, 1988, Unit 1 tripped from 72% power due to an
, leakage, reactor vessel inner seal leakage, and steam dump packing
                                                          electrical ground in the main generator stator. During the forced
leakage were encountered and properly resolved.
                                                          outage to repair the generator stator, repairs to leaking steam
On ' November. 6,1988, Unit 1 entered Mode 2 and went critical .
                                                          generator safety valves and a pressurizer safety valve were also
On
                                                          accomplished.                         ,
November 10, 1988, Unit 1 entered Mode
                                                          On December 25,1988, Unit 1 achieved criticality, entered Mode 1,
1,
                                                          the generator was synchronized with the grid, and power escalation
the generator was
                                                          began.
synchronized with the grid, and power escalation began.
                                                          On December 26,1988, Unit 1 tripped on low-low level in #4 steam
Several
                                                          generator.   The trip was caused by a series of events that started
personnel errors related to equipment surveillance
                                                          with a manual trip of the turbine due to generator seal rubbing.
caused ESF
                                                          After the turbine trip, steam generator level was controlled using
actuations while in Modes 2 and 1.
                                                          manual feedwater control which resulted in a feerwater isolation from
On November 18, 1988, Unit 1 tripped from 72% power due to an
                                                          high-high level in #2 steam generator followed by the reactor trip on
electrical ground in the main generator stator.
                                                          low-low level in #4 steam generator.
During the forced
                                                          On December 27,1988, Unit 1 achieved criticality and began power
outage to repair the generator stator, repairs to leaking steam
                                                          escalation. On December 30, 1988, Unit I achieved 98% reactor power.
generator safety valves and a pressurizer safety valve were also
                                                          On January 19, 1989, Unit 2 was shutdown to begin the s heduled cycle
accomplished.
                                                          3 refueling outage after 210 continuous days of operation.
,
On December 25,1988, Unit 1 achieved criticality, entered Mode 1,
the generator was synchronized with the grid, and power escalation
began.
On December 26,1988, Unit 1 tripped on low-low level in #4 steam
generator.
The trip was caused by a series of events that started
with a manual trip of the turbine due to generator seal rubbing.
After the turbine trip, steam generator level was controlled using
manual feedwater control which resulted in a feerwater isolation from
high-high level in #2 steam generator followed by the reactor trip on
low-low level in #4 steam generator.
On December 27,1988, Unit 1 achieved criticality and began power
escalation.
On December 30, 1988, Unit I achieved 98% reactor power.
On January 19, 1989, Unit 2 was shutdown to begin the s heduled cycle
3 refueling outage after 210 continuous days of operation.
s
s
        ._.-__m___                 _ _ . _ _ _ _ . _ .
._.-__m___
_ _ . _ _ _ _ . _ .


                                                                                  . _ _ _ _ _ . _ _ - _ _ _ _ _ - _ _
. _ _ _ _ _ . _ _ - _ _ _ _ _ - _ _
  ,
4
      4
,
    4~
4~
-                                                       5
5
                  B. Direct-Inspection and Review Activities
-
                      During the assessment period, routine inspections were performed at
B.
                      the Sequoyah facility by the NRC. staff. Special inspections were
Direct-Inspection and Review Activities
                          -
During the assessment period, routine inspections were performed at
                      conducted as follows.:
the Sequoyah facility by the NRC. staff.
                      -      February 4~- June 25, 1988; a series of special inspections.cf
Special inspections were
                            the Unit 2 heatup and restart effort were conducted by the NRC
-
                            Sequoyah Restart Task Force. These inspections included control
conducted as follows.:
                            room observation and reviews of activities associated with the
February 4~- June 25, 1988; a series of special inspections.cf
                            restart effort. (88-02,88-17,88-20,88-22,88-26,88-28,88-34)
-
                                                                                                                        ~
the Unit 2 heatup and restart effort were conducted by the NRC
                      -      February 1-19, 1988; a special inspection was performed to
Sequoyah Restart Task Force.
                            assess the corrective actions performed by TVA in response to
These inspections included control
                            the findings of the Integrated Design Inspection. (88-13)
room observation and reviews of activities associated with the
                      -
restart effort. (88-02,88-17,88-20,88-22,88-26,88-28,88-34)
                            February 8-12, 1988; a special inspection was conducted to
~
                            assure that the licensee's corrective action program implementa-
February 1-19, 1988; a special inspection was performed to
                            tion adequately dispositioned adverse conditions, including
-
                            generic issues. (88-15)
assess the corrective actions performed by TVA in response to
                      -      February 15-19, 1988; a special inspection of the open restart
the findings of the Integrated Design Inspection. (88-13)
                              issues' in the civil engineering area was conducted to determine
-
                            that adequate corrective action and resolution had occurred to
February 8-12, 1988; a special inspection was conducted to
                            support the restart of Unit 2. (88-12)
assure that the licensee's corrective action program implementa-
                                                                                                                      '
tion adequately dispositioned adverse conditions, including
                      -      February 29 - March 4, 1988; a special operational readiness
generic issues. (88-15)
                              inspection was conducted to assess the adequacy of the
February 15-19, 1988; a special inspection of the open restart
                              licensee's preparations for Unit 2 restart. (88-16)
-
                      -      March 14-23, 1988; a special fire protection inspection was
issues' in the civil engineering area was conducted to determine
                            conducted for Unit 2 restart in the area of implementation of
that adequate corrective action and resolution had occurred to
                              the' requirements of 10 CFR 50 Appendix R, Sections III.G, III.J.                           l
support the restart of Unit 2. (88-12)
                                                                                                                          '
'
                              III.L, and 111.0 including safe shutdown logic. (88-24)
February 29 - March 4, 1988; a special operational readiness
                      -
-
                              June 20 - July 8,     1988; a special Safety System Quality
inspection was conducted to assess the adequacy of the
                              Evaluation vertical slice review was conducted on the                                       j
licensee's preparations for Unit 2 restart. (88-16)
                              Containment Spray System to assess the licensee's Nuclear
March 14-23, 1988; a special fire protection inspection was
                              Performance Plan implementation for Unit I restart. (88-29)
-
                      -      July 11-15 and August 23-24, 1988; a special inspection was
conducted for Unit 2 restart in the area of implementation of
                              conducted to assess the effect of excessive cooldowns following
the' requirements of 10 CFR 50 Appendix R, Sections III.G, III.J.
                              reactor trips on end-of-life shutdown margin. (88-35)
l
                      -
'
                            ' July 25-28, 1988; a special fire protection inspection was
III.L, and 111.0 including safe shutdown logic. (88-24)
                              conducted for Unit 1 restart in the area of implementation of
-
                              the requirements of 10 CFR 50 Appendix R, Sections III.G, III.J,
June 20 - July 8,
                              III.L, and 111.0 including safe shutdown logic. (88-37)
1988; a special Safety System Quality
                      -
Evaluation vertical slice review was conducted on the
                              August 29 - September 2,1908; a special operational readiness
j
                              inspection was conducted to assess the adequacy of the
Containment Spray System to assess the licensee's Nuclear
                              licensee's preparations for Unit 1 restart. (88-42)
Performance Plan implementation for Unit I restart. (88-29)
        _ _ - _ _
July 11-15 and August 23-24, 1988; a special inspection was
-
conducted to assess the effect of excessive cooldowns following
reactor trips on end-of-life shutdown margin. (88-35)
-
' July 25-28, 1988; a special fire protection inspection was
conducted for Unit 1 restart in the area of implementation of
the requirements of 10 CFR 50 Appendix R, Sections III.G, III.J,
III.L, and 111.0 including safe shutdown logic. (88-37)
-
August 29 - September 2,1908; a special operational readiness
inspection was conducted to assess the adequacy of the
licensee's preparations for Unit 1 restart. (88-42)
_ _ - _ _


              _ - _ _ - _ _ _ -     _ _ . .   . _ - _ -
_ - _ _ - _ _ _ -
        6 3'
_ _ . .
. _ - _ -
6 3'
,
,
  ,.
,.
                    9
9
  '                                                                           6
'
                                  -        September 6-9, 1988; a special inspection was conducted to
6
                                            assess the licensee's unreviewed safety question determination
September 6-9, 1988; a special inspection was conducted to
                                            program and implementation. (88-43)
-
                                  -        September 25 - November 21, 1988; a series of special inspec-
assess the licensee's unreviewed safety question determination
                                            tions of the Unit I heatup and restart effort were conducted by
program and implementation. (88-43)
                                            the NRC Sequoyah Restart Task Force. These inspections included
September 25 - November 21, 1988; a series of special inspec-
                                            control room observation and reviews of activities associated
-
                                            with the restart effo-t. (88-40,88-46,88-47,88-48,88-49,88-51,
tions of the Unit I heatup and restart effort were conducted by
                                            88-52,88-55)
the NRC Sequoyah Restart Task Force.
                                  -        December 12, 1988 - January 26, 1989; a special ' quality
These inspections included
                                            verification inspection was conducted in the areas of
control room observation and reviews of activities associated
                                            maintenance, modifications, operations, radwaste processing, and
with the restart effo-t. (88-40,88-46,88-47,88-48,88-49,88-51,
                                -
88-52,88-55)
                                            correctiveactions.(88-50)
December 12, 1988 - January 26, 1989; a special ' quality
                                  The staff spent more effort on Sequoyah than on any other operating
-
                                  plant and also expended more effort than 'during the basis period.
verification inspection was conducted in the areas of
                                  Reviews by the staff included TVA's Corporate and Sequoyah Nuclear
maintenance, modifications, operations, radwaste processing, and
                                  Performance Plan (NPP) programs; the Employee Concern Task Group
-
                                  (ECTG) element reports; sixty-five amendments to the Unit 1 and 2
correctiveactions.(88-50)
                                  Technical Specifications including an exigent amendment, an emergency
The staff spent more effort on Sequoyah than on any other operating
                                  amendment, and a waiver of compliance; and four exemptions. The NPP
plant and also expended more effort than 'during the basis period.
                                  reviews were documented in the NRC Safety Evaluation Report
Reviews by the staff included TVA's Corporate and Sequoyah Nuclear
                                  NUREG-1232 Volume 1 and 2 and its supplement, and included reviews in
Performance Plan (NPP) programs; the Employee Concern Task Group
                                  the major areas of adequacy of design, special programs, restart
(ECTG) element reports; sixty-five amendments to the Unit 1 and 2
                                  readiness, employee concerns, and allegations.                 The areas of adecuacy
Technical Specifications including an exigent amendment, an emergency
                                  of design, special programs, and restart readiness were further
amendment, and a waiver of compliance; and four exemptions.
                                  . broken down as follows:
The NPP
                                            Adequacy of Design
reviews were documented in the NRC Safety Evaluation Report
                                            1.           Plant Modification and Design Control
NUREG-1232 Volume 1 and 2 and its supplement, and included reviews in
                                            2.           Design Baseline Verification Program
the major areas of adequacy of design, special programs, restart
                                            3.           Design Calculations Program
readiness, employee concerns, and allegations.
                                            4.           Alternately Analyzed Piping and Supports
The areas of adecuacy
                                            5.           Cable Tray Supports
of design, special programs, and restart readiness were further
                                            6.           Concrete Quality
. broken down as follows:
                                            7.           Miscellaneous Civil Engineering Calculations
Adequacy of Design
                                            Special Programs
1.
                                                                                                                        l
Plant Modification and Design Control
                                            1.           Fire Protection                                               i
2.
                                            2.           Environmental Qualification of Electrical Equipment
Design Baseline Verification Program
                                                            Important to Safety
3.
                                            3.           Piece Part Qualification (Procurement)
Design Calculations Program
                                            4.           Sensing Line Issues
4.
                                            5.           Welding                                                       .
Alternately Analyzed Piping and Supports
                                                                                                                        '
5.
                                            6.           Containment Isolation
Cable Tray Supports
                                            7.           Contair, ment Coatings                                       l
6.
                                                                                                                        l
Concrete Quality
                                                                                                                        l
7.
                                                                                                                        l
Miscellaneous Civil Engineering Calculations
                                                                                                                        l
Special Programs
  _ _ _ _ _ . . _ _ _
l
1.
Fire Protection
i
2.
Environmental Qualification of Electrical Equipment
Important to Safety
3.
Piece Part Qualification (Procurement)
4.
Sensing Line Issues
5.
Welding
.
'
6.
Containment Isolation
7.
Contair, ment Coatings
l
l
l
l
l
_ _ _ _ _ . . _ _ _


            -     _   _
-
                                      _
_
    .
_
        .
_
L     .
.
.
L
e
e
[ :.                                                         7
.
                              '8.       Moderate-Energy Line Breaks
[ :.
                              9.-     ECCS Water Loss Outside Crane Wall / Air Return Fan
7
                                          0perability
'8.
Moderate-Energy Line Breaks
9.-
ECCS Water Loss Outside Crane Wall / Air Return Fan
0perability
i
10.
Platform Thermal Growth
11.
Pipe Wall Thinning Assessment
12.
Cable Installation
13.
Fuse Replacement
Restart Readiness
1.
Operational Readiness
2.
Management
3.
Quality Assurance
4.
Operating Experience Improvement
5.
Post-Modification Testing
6.
Surveillance Instruction Review
7.
Operability "Look Back"
8.
Maintenance
9.
Restart Test Program
!
10.
Training
11. Security
1~2 .
Emergency Preparedness
13.
Radiological Controls
14.
Restart Activities List
II. . SUMMARY OF RESULTS-
,
' A' comparison of the present SALP ratings to the previous SALP ratings cf 4
years ago (1984 to 1985) would be of little benefit in determining the
current trend of the licensee.
In order to evaluate the current trend cf
the licensee from the
reassessment period to the assessment period, an
additional summary is provided below of the NRC staff evaluation for the
period from January 1,1987 until the start of the assessment period
(February 4,1988) to be used as a basis for comparison.
The' NRC established an Office of Special Projects (0SP) in February 1987
to address the particularly complex regulatory problems of TVA and one other
utility.
Part of the OSP goal was to assess whether identified problems
to the licensee were on a path to an acceptable solution, and where not,
to identify acceptable solutions necessary to enable the staff to complete
its licensing reviews of these facilities, consistent with the NRC's
statutory mandate to protect the health and safety of the public.
A.
Basis Period Summary (January 1,1987 - February 3,1988)
1.
Plant Operations
During the entire basis period both units were in the shutdown
mode.
Weaknesses were identified in the adequacy of Abnormal
and Emergency Operating procedures, emergency contingency action
procedures, compensatory operator actions,
configuration
i
i
                              10.      Platform Thermal Growth
                              11.      Pipe Wall Thinning Assessment
                              12.      Cable Installation
                              13.      Fuse Replacement
                              Restart Readiness
                                1.      Operational Readiness
                              2.      Management
                              3.      Quality Assurance
                              4.      Operating Experience Improvement
                              5.      Post-Modification Testing
                              6.      Surveillance Instruction Review
                                7.      Operability "Look Back"
                              8.      Maintenance
                                        Restart Test Program                                          !
                                9.
                                10.    Training
                                11. Security
                                1~2 .  Emergency Preparedness
                                13.    Radiological Controls
                                14.    Restart Activities List
        II. . SUMMARY OF RESULTS-                                                          ,
                ' A' comparison of the present SALP ratings to the previous SALP ratings cf 4
                years ago (1984 to 1985) would be of little benefit in determining the
                  current trend of the licensee.            In order to evaluate the current trend cf
                  the licensee from the reassessment period to the assessment period, an
                  additional summary is provided below of the NRC staff evaluation for the
                  period from January 1,1987 until the start of the assessment period
                    (February 4,1988) to be used as a basis for comparison.
                  The' NRC established an Office of Special Projects (0SP) in February 1987
                  to address the particularly complex regulatory problems of TVA and one other
                  utility.    Part of the OSP goal was to assess whether identified problems
                  to the licensee were on a path to an acceptable solution, and where not,
                    to identify acceptable solutions necessary to enable the staff to complete
                    its licensing reviews of these facilities, consistent with the NRC's
                  statutory mandate to protect the health and safety of the public.
                  A.      Basis Period Summary (January 1,1987 - February 3,1988)
                          1.  Plant Operations
                                During the entire basis period both units were in the shutdown
                                mode.      Weaknesses were identified in the adequacy of Abnormal
                                and Emergency Operating procedures, emergency contingency action
                                procedures, compensatory operator actions, configuration
                                                                                                      i


    ,
(.
        (.
,
      4i
4i
  .
.
                                    8     ,                                   .
8
                                                                                i
,
                                                                                t
.
            control, the clearance process, investigation and resolution of     i
i
            event related issues, . involvement of first line and upper level   j
t
            management in the day-to-day operation of the plant, and control   j
control, the clearance process, investigation and resolution of
            and authority over plant activiMes impacting schedule. Some         !
i
            deportability / operability determinatices were classified as
event related issues, . involvement of first line and upper level
            unknown while awaiting Division of Nut ear
j
                                                    l  Engineering (DNE)
management in the day-to-day operation of the plant, and control
            review which was not always t;mely or responsive. In addition,
j
            there was a reluctance by the licensee to report items that they
and authority over plant activiMes impacting schedule. Some
            felt were minor. As a result, several events were nct properly
!
            classified and repneted.   Material condition, drawing adequacy
deportability / operability determinatices were classified as
            and configuration management training were acceptable.
unknown while awaiting Division of Nut ear Engineering (DNE)
            These issues indicated a lack of management attention to and
l
            involvement in the operational aspects of the plant. Control
review which was not always t;mely or responsive.
            room operators were burdened with the work control management
In addition,
            function.   Their decisions in controlling these activities were
there was a reluctance by the licensee to report items that they
            often reversed by management.     This resulted in limiting the
felt were minor.
            amount of time senior reactor operators spent in the plant, a
As a result, several events were nct properly
            reduction in the amount of time reactor operators spent
classified and repneted.
            observing control panel indications, and a feeling that
Material condition, drawing adequacy
            management did not respect their ability to make decisions.
and configuration management training were acceptable.
            Several management changes occurred during the basis period
These issues indicated a lack of management attention to and
            which contributed to major improvements.in plant activities. The
involvement in the operational aspects of the plant.
            new managers included the Deputy Site Director, Plant Manager,
Control
            Operations Superintendent, and Corporate Outage / Maintenance
room operators were burdened with the work control management
function.
Their decisions in controlling these activities were
often reversed by management.
This resulted in limiting the
amount of time senior reactor operators spent in the plant, a
reduction in the amount of time reactor operators spent
observing control panel indications, and a feeling that
management did not respect their ability to make decisions.
Several management changes occurred during the basis period
which contributed to major improvements.in plant activities. The
new managers included the Deputy Site Director, Plant Manager,
Operations Superintendent, and Corporate Outage / Maintenance
'
'
            Managers.
Managers.
            The operations section was adequately staffed to suppnrt piant
The operations section was adequately staffed to suppnrt piant
            operations. ' Control room and plant shif t rotation was increased
operations. ' Control room and plant shif t rotation was increased
            to a six shift rotation late in the basis period.     Overtime wcs
to a six shift rotation late in the basis period.
            routinely used to augment normal shift staffing with several
Overtime wcs
            occasions identified where administrative limits were exceeded
routinely used to augment normal shift staffing with several
            without receiving prior plant manager approval. The 1987 i;RC
occasions identified where administrative limits were exceeded
            replacement examinations for licensed operators indicated
without receiving prior plant manager approval.
            satisfactory results (5 out of 5 passed).
The 1987 i;RC
            Measures were implemented to revise and control primary drawings
replacement examinations for licensed operators indicated
            in the control room.     These drawings were redrawn and
satisfactory results (5 out of 5 passed).
            maintained by computer-aided drafting systems which resulted in
Measures were implemented to revise and control primary drawings
            improved accuracy and a more timely revision process. System
in the control room.
            logic drawings.were removed from the primary drawing list during
These drawings were redrawn and
            1986 because they were not routinely updated and revised as
maintained by computer-aided drafting systems which resulted in
            plant systems were modified.
improved accuracy and a more timely revision process.
            Procedural compliance by Operations personnel was judged to be
System
            marginally better than the plant staff as a whole. Instances of
logic drawings.were removed from the primary drawing list during
            procedure deviations and non-compliances occurred at an
1986 because they were not routinely updated and revised as
            unacceptable frequency, and resulted in several reportable
plant systems were modified.
            events.
Procedural compliance by Operations personnel was judged to be
                                                                              i
marginally better than the plant staff as a whole.
Instances of
procedure deviations and non-compliances occurred at an
unacceptable frequency, and resulted in several reportable
events.
i


                                                                                                  , - --- q
, - --- q
                                                                    ~
~
                                                                                                            .
'
                    '
.
  .
.
) ..
)
  *                                                       9
..
                              .The licensee made considerable progress in resolving the several
*
                                hundred technical issues encountered after the 1985 shutdown of
9
                                both units. Issues that remained to be resolved at the end of
.The licensee made considerable progress in resolving the several
                                the basis period included the evaluation of containment sump
hundred technical issues encountered after the 1985 shutdown of
                                level transmitters, lower containment coolers, and Senior
both units.
                                Operator manning.
Issues that remained to be resolved at the end of
                          2.   Radiological Controls
the basis period included the evaluation of containment sump
                                Inspections conducted during the basis period of the Sequoyah
level transmitters, lower containment coolers, and Senior
                                radiation protection program, indicated that the actions taken
Operator manning.
                                by the licensee, including correction of previous weaknesses in
2.
                                its program for maintaining exposure as-low-as-reasonably-
Radiological Controls
                                achievable (ALARA), were sufficient to support plant restart.
Inspections conducted during the basis period of the Sequoyah
                                One significant event involved an exothermic reaction during a
radiation protection program, indicated that the actions taken
                                radwaste solidification process which caused personnel
by the licensee, including correction of previous weaknesses in
                                contaminations and higher than expected radiation levels.
its program for maintaining exposure as-low-as-reasonably-
                                Considerable organizational changes had taken place in the
achievable (ALARA), were sufficient to support plant restart.
                                Chemistry Group during the period. These revisions assured
One significant event involved an exothermic reaction during a
                                close management involvement in maintenance of quality, storage
radwaste solidification process which caused personnel
                                of radioactive waste, and effluent releases. Close coordination
contaminations and higher than expected radiation levels.
                                with the Corporate Chemistry group resulted in resolution of
Considerable organizational changes had taken place in the
                              . technical issues in a timely manner.
Chemistry Group during the period.
                                The organizations were responsive to NRC initiatives in that
These revisions assured
                        ,,      open items were being . closed out as the organization prepared
close management involvement in maintenance of quality, storage
                                for Unit 2 startup. Staffing had been reviewed, and several new
of radioactive waste, and effluent releases.
                                management personnel were added to the Chemistry Group.
Close coordination
                          3.   Maintenance / Surveillance
with the Corporate Chemistry group resulted in resolution of
                                During the SALP basis period the Sequoyah maintenance program
. technical issues in a timely manner.
                                experienced numerous weaknesses.     These weaknesses were in
The organizations were responsive to NRC initiatives in that
                                procedural compliance, corporate maintenance guidcnce,
open items were being . closed out as the organization prepared
                                maintenance trending, root cause analysis, first line manage-
,,
                                ment involvement, training for maintenance planners, work
for Unit 2 startup.
                                control, maintenance coordination, equipment classification
Staffing had been reviewed, and several new
                                (Q-list), maintenance history tracking and trending, mainten-
management personnel were added to the Chemistry Group.
                                ance procedure adequacy, plant drawing use, the preventive
3.
                                maintenance program, accountability of maintenance tools and
Maintenance / Surveillance
                                equipment, post modification testing, quality assurance
During the SALP basis period the Sequoyah maintenance program
                                involvement with maintenance activities, temporary alterations,
experienced numerous weaknesses.
                                and corrective action. In addition, there were significant
These weaknesses were in
                                backlogs .in the modifications, temporary modifications, and
procedural
                                maintenance areas.     There was significant overlap between those
compliance,
                                issues identified by ,the NRC and those issues identified by
corporate maintenance
                                TVA's Nuclea.r Manager's Review Group maintenance inspections.
guidcnce,
                                Tracking, trending and scheduling were improved and craft
maintenance trending, root cause analysis, first line manage-
                                reviews were implemented which improved the quality of mainten-
ment involvement, training for maintenance planners, work
                                ance activities. Areas that did not demonstrate active direction
control, maintenance coordination, equipment classification
      _ _ _ _ _ _ _ _ _
(Q-list), maintenance history tracking and trending, mainten-
ance procedure adequacy, plant drawing use, the preventive
maintenance program, accountability of maintenance tools and
equipment, post modification testing, quality assurance
involvement with maintenance activities, temporary alterations,
and corrective action.
In addition, there were significant
backlogs .in the modifications, temporary modifications, and
maintenance areas.
There was significant overlap between those
issues identified by ,the NRC and those issues identified by
TVA's Nuclea.r Manager's Review Group maintenance inspections.
Tracking, trending and scheduling were improved and craft
reviews were implemented which improved the quality of mainten-
ance activities. Areas that did not demonstrate active direction
_ _ _ _ _ _ _ _ _


                                                                              .-   _ _ _ - _ _ _ _ - _ _ -
.-
                  .
_ _ _ - _ _ _ _ - _ _ -
            , _
, _
          . .
.
      - ..
. .
                                                10
- ..
                      during the basis period were the maintenance instruction
10
                      enhancement project which was resolved during the SALP
during the basis period were the maintenance instruction
                      assessment period,' and composite maintenance crews which were
enhancement project which was resolved during the SALP
                      identified by the Nuclear Maintenance Review Grcup (NMRG) as
assessment period,' and composite maintenance crews which were
                      having implementation problems but were not acted upon by TVA
identified by the Nuclear Maintenance Review Grcup (NMRG) as
                    . management.     Institute for Nuclear Power Operations (INP0)
having implementation problems but were not acted upon by TVA
                      accreditation of the training for nine previously selected
. management.
                      maintenance craft areas was received during the SALP basis
Institute for Nuclear Power Operations (INP0)
                      period.
accreditation of the training for nine previously selected
                      The NRC identified significant problems in the area of procure-
maintenance craft areas was received during the SALP basis
                      ment of safety-related parts and equipment at Sequoyah and was                       '
period.
                      considering escalated enforcement action. Based on the NRC
The NRC identified significant problems in the area of procure-
                      findings, TVA in general and Sequoyah in particular initiated an
ment of safety-related parts and equipment at Sequoyah and was
                      extensive Replacement Items Program (RIP) to ensure that
'
                      appropriate parts and equipment were installed in the plant for
considering escalated enforcement action.
                      EQ and seismic qualification of equipment prior to the restart
Based on the NRC
                      of the Sequoyah units. This included training in repair part
findings, TVA in general and Sequoyah in particular initiated an
                      and procurement control which was considered one of the causes                       .
extensive Replacement Items Program (RIP) to ensure that
                      of the problem. Based on the shutdown plant enforcement policy                       I
appropriate parts and equipment were installed in the plant for
                      and successful implementation prior to unit restart, these
EQ and seismic qualification of equipment prior to the restart
                      issues were given discretionary enforcement.   The program also
of the Sequoyah units.
                      established controls to ensure that future procurement of
This included training in repair part
                      safety-related equipment met the appropriate requirements.
and procurement control which was considered one of the causes
                      Sequoyah was completing the documentation and field work for ,
.
                      their EQ program. Sequoyah was found to have an excellent EQ
of the problem.
                      program which had proper management attention ard proposed sound
Based on the shutdown plant enforcement policy
                      technical resolutions as problems arose.     TVA management was
I
                      found to be knowledgeable of NRC and industry standards and
and successful implementation prior to unit restart, these
                      requirements in this area.
issues were given discretionary enforcement.
                      Licensee management recognized that storage of equipment did not
The program also
                    -meet the requirements of American National Standard Institute
established controls to ensure that future procurement of
                      (ANSI) 45.2.2 and initiated an improvement program to correct
safety-related equipment met the appropriate requirements.
                      this problem. The' equipment storage upgrade program initiated
Sequoyah was completing the documentation and field work for ,
                      by licensee management was adequate and well implemented.   The
their EQ program.
                      implementation included a computerized tracking system to                             ,
Sequoyah was found to have an excellent EQ
                      identify the exact location of each part, and well organized,                       i
program which had proper management attention ard proposed sound
                      clearly marked storage areas that met the ANSI 45.2.2 storage
technical resolutions as problems arose.
                      class requirements, even at remote on-site locations. At the
TVA management was
                      close of the SALP tasis period safety related component storage
found to be knowledgeable of NRC and industry standards and
                      was in excellent condition, as a result of several energetic
requirements in this area.
                      knowledgeable managers who were personally involved in the
Licensee management recognized that storage of equipment did not
                      resolution of this industry wide issue.
-meet the requirements of American National Standard Institute
                      As a resul t of significant NRC concerns with surveillance
(ANSI) 45.2.2 and initiated an improvement program to correct
                      instruction inadequacies which were under consideration for
this problem.
                      escalated enforcement, the licensee established a surveillance
The' equipment storage upgrade program initiated
                      instruction review team to compare existing surveillance                             i
by licensee management was adequate and well implemented.
                      instructions to TS surveillance requirements.     This review                       1
The
                                                                                                            i
implementation included a computerized tracking system to
                                                                                                              ,
,
_____..u__     -
i
identify the exact location of each part, and well organized,
clearly marked storage areas that met the ANSI 45.2.2 storage
class requirements, even at remote on-site locations.
At the
close of the SALP tasis period safety related component storage
was in excellent condition, as a result of several energetic
knowledgeable managers who were personally involved in the
resolution of this industry wide issue.
As a resul t of significant NRC concerns with surveillance
instruction inadequacies which were under consideration for
escalated enforcement, the licensee established a surveillance
instruction review team to compare existing surveillance
i
instructions to TS surveillance requirements.
This review
1
i
,
_____..u__
-


                                                                                . _ - . _ _ _ _ -
. _ - . _ _ _ _ -
      . s.
. s.
    ,
,
    .
.
                                              11
11
                      effort identified.a significant number of additiona! issues that
effort identified.a significant number of additiona! issues that
                      resulted in approximately 15 Licensee Event Reports (LERs) being
resulted in approximately 15 Licensee Event Reports (LERs) being
                      written.   A number of significant revisions and management
written.
                      changes were inade to' the surveillance instruction review and
A number of significant revisions and management
                      update program to achieve technically adequate surveillance
changes were inade to' the surveillance instruction review and
                      instructions that met the surveillance requirements. Management
update program to achieve technically adequate surveillance
                      involvement in the final effort was aggressive and included an
instructions that met the surveillance requirements. Management
                      independent validation process which wcs particularly well
involvement in the final effort was aggressive and included an
l                     managed and ensured that the surveillance instructions produced
independent validation process which wcs particularly well
                      were of high quality and technically adequate. Based on the
l
                      shutdown plant enforcement policy and implementation of an
managed and ensured that the surveillance instructions produced
                      acceptable surveillance program prior to restart, these issues
were of high quality and technically adequate.
                      were given discretionary enforcement.                                             i
Based on the
                      The licensee established a Nuclear Performance Plan Restart Test
shutdown plant enforcement policy and implementation of an
                      Program in order to ensure the operability of scfety related                     ,
acceptable surveillance program prior to restart, these issues
                      equipment which had been modified.   A review matrix of component.               i
i
                      functions and previous",y performed surveillance was established                 '
were given discretionary enforcement.
                      to ensure the testing of functions that had not been tested.
The licensee established a Nuclear Performance Plan Restart Test
                      This program was considered adequately staffed with trained
Program in order to ensure the operability of scfety related
                      individuals and was determined to be acceptable. Only the
,
                      closure of Mode 3 and 2 related items was deferred into the SALP
equipment which had been modified.
                      period.
A review matrix of component.
                      A problem was identified in the Inservice Test (IST) valve test
i
                      program in that essentially all category A and B valves were
functions and previous",y performed surveillance was established
                    ~ included in one Surveillance Instruction (SI) and scheduling was
'
                    . based on the issue date for the SI package, not the test date
to ensure the testing of functions that had not been tested.
                      for individual valves in the package.       The test dates for
This program was considered adequately staffed with trained
                      individual valves were not controlled resulting in a number of
individuals and was determined to be acceptable.
                      valves exceeding their. test frequency.                                           ,
Only the
                                                                                                      i
closure of Mode 3 and 2 related items was deferred into the SALP
                      Procedural adherence was a weakness which contributed to several                 !'
period.
                      events and enforcement actions and indicated a lack of manage-
A problem was identified in the Inservice Test (IST) valve test
                      ment involvement in and attention to this area. In addition,
program in that essentially all category A and B valves were
                      corrective actions were not effective in reducing the results of
~ included in one Surveillance Instruction (SI) and scheduling was
                      this weakness until well into the SALP assessment period.
. based on the issue date for the SI package, not the test date
                      Conduct of testing was identified as an area of weakness during                 !
for individual valves in the package.
                      the activities leading up to the restart of Unit 2.                   The
The test dates for
                      licensee took strong corrective action with the issuance of
individual valves were not controlled resulting in a number of
                      special conduct of testing administrative controls which
valves exceeding their. test frequency.
                      resulted in a significant improvement in plant operations.
,
                      The effectiveness of the short term layup of the steam and power
i
                      conversion system (the secondary water system) was adversely
Procedural adherence was a weakness which contributed to several
                      affected due to uncertainties in the startup schedule.                     The
!
                      uncertainties were directly related, to the inability of
'
                      management to control restart activity schedules. Continuous
events and enforcement actions and indicated a lack of manage-
                      maintenance and modifications of systems created a condition
ment involvement in and attention to this area.
                                                        ~
In addition,
                      where the desired controls did not in some cases maintain the
corrective actions were not effective in reducing the results of
                                    -
this weakness until well into the SALP assessment period.
  !
!
          _ _ . . _
Conduct of testing was identified as an area of weakness during
the activities leading up to the restart of Unit 2.
The
licensee took strong corrective action with the issuance of
special conduct of testing administrative controls which
resulted in a significant improvement in plant operations.
The effectiveness of the short term layup of the steam and power
conversion system (the secondary water system) was adversely
affected due to uncertainties in the startup schedule.
The
uncertainties were directly related, to the inability of
management to control restart activity schedules.
Continuous
maintenance and modifications of systems created a condition
where the desired controls did not in some cases maintain the
~
-
!
_ _ . . _


                - - .
- - .
                              .
.
            ,.
,.
              .
.
          "
"
                                                            12
12
                                  parameters for minimizing corrosion and degradation of the
parameters for minimizing corrosion and degradation of the
                                  car''1 steel systems.     The licensee was responsive to NRC
car''1 steel systems.
                                  cor   ms expressed during inspections and to NRC information
The licensee was responsive to NRC
                                  not   a.   Actions were taken to enhance the pro,tection of
cor
                                  systems .during the extended short term layup.
ms expressed during inspections and to NRC information
                                  Organizational changes in the water chemistry program were a
not
                                  strengthening factor for water chemistry control. Qualifica-
a.
                                  tions of the chemistry management and staff were adequate with a
Actions were taken to enhance the pro,tection of
                                  sufficient number of chemists and analysts to maintain chemistry
systems .during the extended short term layup.
                                  control.     Other elements of the water chemistry progran
Organizational changes in the water chemistry program were a
          '
strengthening factor for water chemistry control.
                                  (procedures, training, and equipment) were maintained at a
Qualifica-
                                  sufficient level to achieve chemistry control during plant
tions of the chemistry management and staff were adequate with a
                                  startup.
sufficient number of chemists and analysts to maintain chemistry
                                  During the basis period the licensee made progress in changing
control.
                                  its maintenance philosophy from reactive to preventive and was
Other elements of the water chemistry progran
                                  trying to reinforce procedural compliance.
(procedures, training, and equipment) were maintained at a
                                4. Emeroency Preparedness
'
                                  The Emergency Preparedness program was adequately maintained
sufficient level to achieve chemistry control during plant
                                  during the basis period.       Two routine inspections and an
startup.
                                  emergency exercise indicated the. licensee was maintaining an
During the basis period the licensee made progress in changing
                                  effective emergency preparedness program. Licensee management
its maintenance philosophy from reactive to preventive and was
        -
trying to reinforce procedural compliance.
                                  attention to the program was adequate         The two violations
4.
                                  identified during the rcutine inspections oddressed an
Emeroency Preparedness
                                  inadequacy in the training for licensed operators and a failure
The Emergency Preparedness program was adequately maintained
                                  to conduct required monthly concunications checks fcr three
during the basis period.
                                  months.
Two routine inspections and an
                                5. Security
emergency exercise indicated the. licensee was maintaining an
                                  Four routine' security inspections, one material control
effective emergency preparedness program.
                                                                                                      '
Licensee management
                                  inspection and two special inspections relative to Fitness for
attention to the program was adequate
                                  Duty and pre-employment screening were conducted.         Two
The two violations
                                  violations were tited for failure to adequately post a
-
                                  compensatory officer, and for failure to maintain a bullet-
identified during the rcutine inspections oddressed an
                                  resistant barrier. The Fitness for Duty program was judged
inadequacy in the training for licensed operators and a failure
                                  adequate with both a few noteable strengths and one significant
to conduct required monthly concunications checks fcr three
                                  weakness.   The NRC exercised discretionary enforcement in not
months.
                                  issuing a violation regarding numerous pre-employment screening
5.
                                  errors due to the significant corrective action initiated and
Security
                                  that the program was examined and determined acceptable prior to
Four routine' security inspections, one material control
                                  plant startup.     During this period the licensee, although
'
                                  non-operational, did not reduce its security program nor did it
inspection and two special inspections relative to Fitness for
                                  "de\ italize" any of its security areas.       The NRC inspection
Duty and pre-employment screening were conducted.
                                  proc, ram also included various allegations, Employee Concerns and
Two
                                  the licensee's Regulatory Improvement Plan.
violations were tited for failure to adequately post a
                                                                                                      ;
compensatory officer, and for failure to maintain a bullet-
                                                                                                        :
resistant barrier.
                                                                                                      I
The Fitness for Duty program was judged
                                                                                                      !
adequate with both a few noteable strengths and one significant
weakness.
The NRC exercised discretionary enforcement in not
issuing a violation regarding numerous pre-employment screening
errors due to the significant corrective action initiated and
that the program was examined and determined acceptable prior to
plant startup.
During this period the licensee, although
non-operational, did not reduce its security program nor did it
"de\\ italize" any of its security areas.
The NRC inspection
proc, ram also included various allegations, Employee Concerns and
the licensee's Regulatory Improvement Plan.
;
:
I
!
. _ _ - _ _ _ _ _ _ - - _ _ _
. _ _ - _ _ _ _ _ _ - - _ _ _


          - __-
-
''
__-
          .
''
      ,.
.
                                                                                        <
,.
      ..
<
    ~
. .
                                              13
13
                    A licensee Quality Assurance -Audit (QSS-A87-0010) was
~
                    performed and no regulatory issues were raised. With respect to
A licensee Quality Assurance -Audit (QSS-A87-0010) was
                    Safeguards Event Reports, there were four relative to expired     !
performed and no regulatory issues were raised. With respect to
Safeguards Event Reports, there were four relative to expired
!
badges not being voided and various visitor / escort deficiencies.
7_
7_
                    badges not being voided and various visitor / escort deficiencies.
Of the 225 security incident reports per 10 CFR 73.71
n
n
                    Of the 225 security incident reports per 10 CFR 73.71
requirements, the vast majority (nearly 95%) resulted from the
                    requirements, the vast majority (nearly 95%) resulted from the
failure of equipment (hardware and systems) and not human
                    failure of equipment (hardware and systems) and not human
errors.
                    errors.
Midway through this period, the licensee reorganized its
                    Midway through this period, the licensee reorganized its
security organization which resulted in security officers
                    security organization which resulted in security officers
working for and being accountable to ,the Corporate Nuclear
                    working for and being accountable to ,the Corporate Nuclear
Security Support Branch, as oppose to the previous multi-
                    Security Support Branch, as oppose to the previous multi-
management-level structure criticized in prior SALP Reports. A
                    management-level structure criticized in prior SALP Reports. A
new site Security Manager was assigned to the site in July 1987.
                    new site Security Manager was assigned to the site in July 1987.
L
L                   The extended' use of numerous compensatory iaeasures neeGd         !
The extended' use of numerous compensatory iaeasures neeGd
                    because of failed equipment remained the. most significant         l
!
                    regulatory issue throughout this period. ticwever, the licensee
because of failed equipment remained the. most significant
                    was judged as adequately meeting requirements and providing
l
                    security for the facility.                                     -
regulatory issue throughout this period.
                6. Engineering / Technical Support
ticwever, the licensee
                    The licensee's performance in the engineering / technical support
was judged as adequately meeting requirements and providing
                    area was greatly affected by the many changes which were being
security for the facility.
                    experienced by the engineering / technical support staff. Early
-
                    in the baseline perind, the licensee was trying to obtain a
6.
                    clear definition of the scope of effort required to resolve many
Engineering / Technical Support
                    technical and design issues which had been identified through
The licensee's performance in the engineering / technical support
                    licensee sponsored evaluations and audits and NRC inspections;
area was greatly affected by the many changes which were being
                    however, the engineering and technical support staff was
experienced by the engineering / technical support staff.
                    hampered by changes in organization structures and changes in
Early
                    key personnel as well as major changes to the internal
in the baseline perind, the licensee was trying to obtain a
                    engineering procedures.
clear definition of the scope of effort required to resolve many
                    While the above changes hampered early baseline period
technical and design issues which had been identified through
                    performance in engineering / technical support, the licensee had
licensee sponsored evaluations and audits and NRC inspections;
                    - established many special programs to address and resolve
however, the engineering and technical support staff was
                    previously identified issues as well as new issues identified
hampered by changes in organization structures and changes in
                    durug the baseline period (e.g. discrepancies identified during
key personnel as well as major changes to the internal
                    the NRC integrated design inspect''n (IDI)). Some of the issues
engineering procedures.
                    for which special programs had two established included EQ of
While the above changes hampered early baseline period
                      safety-related electrical equipt ~t; design and configuration
performance in engineering / technical support, the licensee had
                    control (design baseline verification program); design
- established many special programs to address and resolve
                    calculations review - electrical, mechanical, nuclear, and
previously identified issues as well as new issues identified
                    civil; electrical     issues; instrument sense line issues;
durug the baseline period (e.g. discrepancies identified during
                      component and piece part qualification; Appendix R; and restart
the NRC integrated design inspect''n (IDI)).
                      testing.
Some of the issues
for which special programs had two established included EQ of
safety-related electrical equipt ~t; design and configuration
control
(design baseline verification program);
design
calculations review - electrical, mechanical, nuclear, and
civil; electrical
issues; instrument sense line issues;
component and piece part qualification; Appendix R; and restart
testing.


_ - _ --                       -   -.
_ - _ --
          .
-
                                                                  -
-.
        ..
-
        .
.
      .
..
                                                                  14
.
                                        The licensee performance in the - engineering / technical support
.
                                        area was satisfactory for some of the programs; however, other
14
                                        programs. were satisfactory only after corrections were made
The licensee performance in the - engineering / technical support
                                        based on NRC input. Examples of programs where the licensee's
area was satisfactory for some of the programs; however, other
                                      . performance was satisfactory and the program implementation was
programs. were satisfactory only after corrections were made
                                        considered acceptable were: EQ; civil calculations; cable tray
based on NRC input.
                                        supports; technical drawings; Design Baseline and Verification
Examples of programs where the licensee's
                                        Program (DBVP); and heat code traceability.
. performance was satisfactory and the program implementation was
                                        Examples of programs where program implementation was initially
considered acceptable were:
                                        considered inadequate included:       component and piece part
EQ; civil calculations; cable tray
                                        qualification (inadequate seismic qualification and dedication
supports; technical drawings; Design Baseline and Verification
                                        of commerciti grade parts for use in safety .c ted equipment);
Program (DBVP); and heat code traceability.
                                        pipe hangers and supports (inacecuate ~ caic id tions and
Examples of programs where program implementation was initially
                                        documentation to demonstrate that installed pipe hangers and
considered inadequate included:
                                        supports met plant design criteria); and instrument sense lines
component and piece part
                                        and instrumentation accuracy calculations (lack of sufficient
qualification (inadequate seismic qualification and dedication
                                        conservatism). While the licensee's implemen :ation of some
of commerciti grade parts for use in safety .c
                                        programs was initially judged to be unsatisfact'ry or inadequate
ted equipment);
                                        relative to engineering / technical support, once problems or
pipe hangers and supports (inacecuate ~ caic i tions and
                                        concerns were identified, the licensee satisfactorily resolved
d
                                        the problems and completed the programs.
documentation to demonstrate that installed pipe hangers and
                                7.     Safety Assessment /Qu'ality Verification
supports met plant design criteria); and instrument sense lines
                                        For the basis period, there was an extensive review effort on
and instrumentation accuracy calculations (lack of sufficient
                                        Sequoyah. The review effort included the following significant
conservatism).
                                        items:                           .
While the licensee's implemen :ation of some
                                        1.   review of the Corporate Nuclear Performance Plan was
programs was initially judged to be unsatisfact'ry or inadequate
                                              completed and NUREG-1232, Volume 1 was issued;
relative to engineering / technical support, once problems or
                                        2.     most of the review of the Sequoyah Nuclear Performance Plan
concerns were identified, the licensee satisfactorily resolved
                                              was completed;
the problems and completed the programs.
                                        3.     most of the Employee Concerns Task Group (ECTG) element
7.
                                              reports on Sequoyah were reviewed;
Safety Assessment /Qu'ality Verification
                                        4.     thirty amendments to the Units 1 and 2 TS were issued; and
For the basis period, there was an extensive review effort on
                                        5.   twenty-one meetings were held with TVA on various technical
Sequoyah.
                                              issues.
The review effort included the following significant
                                        Overall, the work submitted by TVA was reasonably good.     The
items:
                                        submittals generally showed evidence of prior planning by
.
                                        management.     An understanding of the technical issues was
1.
                                        generally !pparent. The resolutions of issues were generally
review of the Corporate Nuclear Performance Plan was
                                        viable, timely, sound and well thought out with conservatism
completed and NUREG-1232, Volume 1 was issued;
                                        exhibited by the licensee's approach. This was generally true
2.
                                        in the basis period except for the issues of cable testing and   ;
most of the review of the Sequoyah Nuclear Performance Plan
                                        the transition of senior nuclear power management from contract
was completed;
                                        employees to permanent employees.
3.
most of the Employee Concerns Task Group (ECTG) element
reports on Sequoyah were reviewed;
4.
thirty amendments to the Units 1 and 2 TS were issued; and
5.
twenty-one meetings were held with TVA on various technical
issues.
Overall, the work submitted by TVA was reasonably good.
The
submittals generally showed evidence of prior planning by
management.
An understanding of the technical issues was
generally !pparent.
The resolutions of issues were generally
viable, timely, sound and well thought out with conservatism
exhibited by the licensee's approach.
This was generally true
in the basis period except for the issues of cable testing and
;
the transition of senior nuclear power management from contract
employees to permanent employees.
l
l
l
l
  .~
.~
            _ . _ . _ _ _ _ _
_ . _ . _ _ _ _ _


, .,
, .,
              ' ''
' ''
,         .
.
    '
,
          ,.
'
                                                                -
,.
                    .
.
      '                                          15-
-
                      -TheLissue of. cable testing which included the issue of-test ing
'
                        10'CFR 50.49 silicone rubber insulated cable which was inside
15-
!"                     containment ; was protracted and- drawn out. .The issue' was -
i
-TheLissue of. cable testing which included the issue of-test ng
10'CFR 50.49 silicone rubber insulated cable which was inside
!"
containment ; was protracted and- drawn out.
.The issue' was -
discussed tnroughout the basis period and was not resolved for
L
L
                      discussed tnroughout the basis period and was not resolved for
'1
'1                     Unit 1 until the! staff letter of- May 25,.1988 in the . rating
Unit 1 until the! staff letter of- May 25,.1988 in the . rating
                        period. ' Die resolution of this issue was not timely and -the
period. ' Die resolution of this issue was not timely and -the
                        technical issues were not well thought out.
technical issues were not well thought out.
        2 .
2 .
E                     The TVA response to the staff's concer.:s on the transition of
E
    ,
The TVA response to the staff's concer.:s on the transition of
                      TVA senior nuclear management was acceptable and the_ safety
TVA senior nuclear management was acceptable and the_ safety
                      - evaluation on the TVA's Corporate Nuclear Performance Plen was
,
                        issued on July 28, 1987; but, TVA was not responsive to the
- evaluation on the TVA's Corporate Nuclear Performance Plen was
                        issues raised ~ by the staff pertaining to the transition from
issued on July 28, 1987; but, TVA was not responsive to the
l                     Jcontract managers to.TVA permanent managers.       As a result, the-
issues raised ~ by the staff pertaining to the transition from
                <
l
                        staff was compelled to request TVA to notify the staff 30 days-
Jcontract managers to.TVA permanent managers.
                        in advance 'of any permanent changes of the senior nuclear
As a result, the-
            ,
,
                      managers.
staff was compelled to request TVA to notify the staff 30 days-
    ..
<
      6             . In Janaery 1987, the NRC approved (for a period of two years)
in advance 'of any permanent changes of the senior nuclear
                      .TVA's Quality Assurance Topical Report', TVA-TR75-1A, Revision 9,
managers.
                        which was; developed to resolve past problems relating to the
..
                        inability of management. to take prompt effective corrective
6
                        action to. prevent recurrence of problems. The past problems
. In Janaery 1987, the NRC approved (for a period of two years)
                        were under consideration for escalated enforcement at the start
.TVA's Quality Assurance Topical Report', TVA-TR75-1A, Revision 9,
                        of the basis period.     During the basis period, Sequoyah began
which was; developed to resolve past problems relating to the
                        implementing the.new topical requirements which involved hiring
inability of management. to take prompt effective corrective
c                      the additional- staff required,' training them to appropriately
action to. prevent recurrence of problems.
                        implement 1the program, and then monitoring the implementation to
The past problems
                        ensure thatithe desired results were achieved. During this
were under consideration for escalated enforcement at the start
                        transition period Sequoyah experienced significant implementa-
of the basis period.
                        tion problems especially with the conditions adverse to quality
During the basis period, Sequoyah began
                      '(CAQR) program which was the subject of several TVA audits and
implementing the.new topical requirements which involved hiring
                      .NRC inspections.     The TVA audits concluded taat the root cause
the additional- staff required,' training them to appropriately
                        of the failure.of theLprogram to not fully process any signif-
c
                        icant CAQRs'was due to a lack of line management and Quality
implement 1the program, and then monitoring the implementation to
                        Assurance (QA) management involvement and attention.       This was
ensure thatithe desired results were achieved.
                        the same reason the previous corrective action program hadn't
During this
                        been effective. Sequoyah responded by deeply involving upper
transition period Sequoyah experienced significant implementa-
                        level managers in the corrective action program implementation.
tion problems especially with the conditions adverse to quality
                        While . problems still existed in the QA program implementation,
'(CAQR) program which was the subject of several TVA audits and
                        the staff concluded that the program began moving in a positive
.NRC inspections.
                        direction toward the end of the basis period after upper level           ;
The TVA audits concluded taat the root cause
                                                                                                '
of the failure.of theLprogram to not fully process any signif-
                        management involvement had significantly increased. Based on             '
icant CAQRs'was due to a lack of line management and Quality
                        the shutdown plant enforcement policy and implementation of an
Assurance (QA) management involvement and attention.
                        acceptable corrective action program prior to restart, the past
This was
                        problems were given' discretionary enforcement.
the same reason the previous corrective action program hadn't
                                                                                            .
been effective.
                        The three ' safety committees which functioned during the basis         f
Sequoyah responded by deeply involving upper
                        period [ Plant Operations Review Committee (PORC), Nuclear Safety         l
level managers in the corrective action program implementation.
                        Review Board (NSRB), Independent Safety Engineering Group                 {
While . problems still existed in the QA program implementation,
  ,
the staff concluded that the program began moving in a positive
                        (ISEG)] went through a change process due to TS changes and               >
direction toward the end of the basis period after upper level
                                                                                              '
;
management involvement had significantly increased.
Based on
'
'
the shutdown plant enforcement policy and implementation of an
acceptable corrective action program prior to restart, the past
problems were given' discretionary enforcement.
.
The three ' safety committees which functioned during the basis
f
period [ Plant Operations Review Committee (PORC), Nuclear Safety
Review Board (NSRB), Independent Safety Engineering Group
{
,
(ISEG)] went through a change process due to TS changes and
>
'
?.
?.
L
L
Line 948: Line 1,291:


, _ _ _ _ _
, _ _ _ _ _
              '                         '
'
            .
'
      ,
.
        .
,
    ~-
.
                                          16
~ -
  f
16
                  charter reviews, which were for the most part a result of NRC
f
                  initiatives.   PORC was initially ineffective, however, improve-
charter reviews, which were for the most part a result of NRC
                  ment-was observed near the end of the basis. period due to both
initiatives.
                  the qualified reviewer TS change and a new plant manager. The
PORC was initially ineffective, however, improve-
                  NSRB and ISEG did not independently identify issues which
ment-was observed near the end of the basis. period due to both
                  produced substantive changes to the site.
the qualified reviewer TS change and a new plant manager.
                  During the basis period, 88 LERs were issued of which 26 were
The
                  classi fied as significant. These resulted primarily from the
NSRB and ISEG did not independently identify issues which
                  design reviews which TVA had initiated.     Some LERs were unclear
produced substantive changes to the site.
                  with respect to the root cause determination of events or
During the basis period, 88 LERs were issued of which 26 were
                  differed from the staff determinations. The licensee esta-
classi fied as significant. These resulted primarily from the
                  blished an ISEG audit, identified similar concerns, and was
design reviews which TVA had initiated.
                  implementing ISEG and NRC recommendations at the end of the
Some LERs were unclear
                  basis period.                                                       j
with respect to the root cause determination of events or
                  Both the Special Employee Concerns Task Group (ECTG) and the new   !
differed from the staff determinations.
                  Employee Concerns Program (ECP) were in existence during the
The licensee esta-
                  basis period. The ECTG was working on resolution of the
blished an ISEG audit, identified similar concerns, and was
                  concerns which it received in the 1985 to early 1986 time frame.   q
implementing ISEG and NRC recommendations at the end of the
                  Numerous revisions to the ECTG reports and their corrective         l
basis period.
                  actions occurred as a result of NRC review. All employee           {
j
                  concerns received during the basis period were processed through
Both the Special Employee Concerns Task Group (ECTG) and the new
                  the ECP. The NRC identified weaknesses relating to resolution
!
                  of generic Lconcerns, administrative issues, and restart
Employee Concerns Program (ECP) were in existence during the
                  determinations which were.promptly addressed and corrected by
basis period.
                  the ECP management. NRC reviews of both programs indicated that
The ECTG was working on resolution of the
                *
concerns which it received in the 1985 to early 1986 time frame.
                                                                                      l
q
                  concerns were being adequately addressed at the end of the basis
Numerous revisions to the ECTG reports and their corrective
                  period.                                                             j
l
                                                                                      l
actions occurred as a result of NRC review.
                  TVA Nuclear Power corporate management was usually involved in
All employee
                  Sequoyah site activities in an effective manner during the basis
{
                  period. There were several management changes at the site which
concerns received during the basis period were processed through
                  contributed to major improvements in operation, security and
the ECP.
                  radiological controls during this period. There were corporate
The NRC identified weaknesses relating to resolution
                  audits made in the radiological controls and maintenance areas
of generic Lconcerns, administrative issues, and restart
                  where actions were taken by corporate management to strengthen
determinations which were.promptly addressed and corrected by
                  these programs. Although many significant problems in programs
the ECP management.
                  at the site were not being identified by TVA prior to NRC
NRC reviews of both programs indicated that
                  inspections, usually strong corrective actions from the corporate '
l
                  level were taken when it was needed to correct the identified
*
                  problems.
concerns were being adequately addressed at the end of the basis
                  For the basis period, corporate management was generally
period.
                  responsive to NRC initiatives. Responses to NRC were generally
j
                  timely and generally sound and thorough. This is shown in the
l
                  significant amount of work completed by the staff and TVA in the
TVA Nuclear Power corporate management was usually involved in
                  basis period.
Sequoyah site activities in an effective manner during the basis
                      ~
period. There were several management changes at the site which
                                                                                      ,
contributed to major improvements in operation, security and
radiological controls during this period.
There were corporate
audits made in the radiological controls and maintenance areas
where actions were taken by corporate management to strengthen
these programs.
Although many significant problems in programs
at the site were not being identified by TVA prior to NRC
inspections, usually strong corrective actions from the corporate
'
level were taken when it was needed to correct the identified
problems.
For the basis period, corporate management was generally
responsive to NRC initiatives.
Responses to NRC were generally
timely and generally sound and thorough.
This is shown in the
significant amount of work completed by the staff and TVA in the
basis period.
~
,
1
1
l
l
t
t


                                                                                                              - . _ _ _ _ _ _ _
-
                                                                                                                                1
. _ _ _ _ _ _ _
                              .
1
  ,
.
    .
,
.
'
'
                                                                      17
17
                                            The staff conducted an inspection of management effectiveness                       1
The staff conducted an inspection of management effectiveness
                                            related to licensing _ activities in the basis period.     The
1
                                            inspection was conducted in key areas of responsibility at both
related to licensing _ activities in the basis period.
                                            the plant site and corporate offices. The staff concluded that
The
                                            corporate management processes in the areas inspected were
inspection was conducted in key areas of responsibility at both
                                            functioning adequately.
the plant site and corporate offices. The staff concluded that
                                  B. Assessment Period Summary (February 4,1988 - February 3,1989)
corporate management processes in the areas inspected were
                                      Sequoyah has been operated in an overall safe manner during the
functioning adequately.
                                      assessment period.     Management involvement in and attention to the
B.
                                      operations and support of the plant has significantly improved as a
Assessment Period Summary (February 4,1988 - February 3,1989)
                                      result of the strong leadership exhibited by the new plant a.anager
Sequoyah has been operated in an overall safe manner during the
                                      and new site director.
assessment period.
                                      The plant operations area matured during the assessment period. After
Management involvement in and attention to the
                                      starting the assessment period with five reactor trips, Unit 2 was on
operations and support of the plant has significantly improved as a
                                      line for 210 continuous days which established a TVA single unit
result of the strong leadership exhibited by the new plant a.anager
                                      record. Unit 1 experienced two reactor trips during startup with
and new site director.
                                      full availability for the rest of the assessment period.     Strengths
The plant operations area matured during the assessment period. After
                                      included the procedures upgrade programs, the emphasis on procedural
starting the assessment period with five reactor trips, Unit 2 was on
                                      compliance, and the ownership concept for the operators. Corrective
line for 210 continuous days which established a TVA single unit
                                      activs for problems once the root cause was identified were consider-
record.
                                      ed a strength. Weaknesses included operation of the radwaste system;
Unit 1 experienced two reactor trips during startup with
                                        -
full availability for the rest of the assessment period.
                                      root cause analysis in relation to the post-trip cooldown shutdown
Strengths
                                      margin issues; and the performance of fire watches. Control of plant
included the procedures upgrade programs, the emphasis on procedural
                                      activities by the control room operators improved during the latter
compliance, and the ownership concept for the operators.
                                      half of the assessment period.
Corrective
                                      The overall. quality and experience level of the health physics staff
activs for problems once the root cause was identified were consider-
                                      is _a program strength, and the licensee's health physics, radwaste,
ed a strength. Weaknesses included operation of the radwaste system;
                                      and chemistry staffing levels are adequate and compare well with
-
                                      other utilities having facilities of similar s,ize.       Management
root cause analysis in relation to the post-trip cooldown shutdown
                                      provides adequate support and is involved in matters related to
margin issues; and the performance of fire watches.
                                      radiation protection.
Control of plant
                                      The maintenance / surveillance area also matured during the assessment
activities by the control room operators improved during the latter
                                      period. Strengths included the leadership exhibited by the new main-
half of the assessment period.
                                      tenance superintendent. the establishment of the work control group,
The overall. quality and experience level of the health physics staff
                                      the establishment of a preventive maintenance upgrade program,
is _a program strength, and the licensee's health physics, radwaste,
                                      implementation of the system and train outage concept for scheduling
and chemistry staffing levels are adequate and compare well with
                                      maintenance, and implementation of the system of the month review
other utilities having facilities of similar s,ize.
                                      program. Weaknesses included the large number of personnel errors or
Management
                                      inadequate procedures which resulted in Engineered Safety Feature or
provides adequate support and is involved in matters related to
                                      reactor protection system actuations; the inability to produce                           ;
radiation protection.
                                      realistic schedules; and the inability to correct problems associated
The maintenance / surveillance area also matured during the assessment
                                                                                                                                '
period. Strengths included the leadership exhibited by the new main-
                            *
tenance superintendent. the establishment of the work control group,
                                      with the feedwater control system.                                                       ,
the establishment of a preventive maintenance upgrade program,
                                M
implementation of the system and train outage concept for scheduling
      _ _ _ _ _ . _ _ _ _ _ _ _
maintenance, and implementation of the system of the month review
program.
Weaknesses included the large number of personnel errors or
inadequate procedures which resulted in Engineered Safety Feature or
reactor protection system actuations; the inability to produce
;
realistic schedules; and the inability to correct problems associated
'
*
with the feedwater control system.
,
M
_ _ _ _ _ . _ _ _ _ _ _ _


__-           - - . .
__-
                                                                                                                                                                              )
- - . .
        -
)
      .                                                                                                                                                                    .l
.
                                                                                                                                                                              !
-
                                                                                                                                                                              '
.
      ..                                                                                                                                                                     j
!
                                                                                                                                                                              i
'
                                                                                                                                                                            1
j
    -
..
                                                            18
i
                      During a full' participation exercise, the licensee demonstrated                                                                                       :'
18
                      that they could satisfactorily respond to an emergency at the
1
                      facility.   However, weaknesses were noted in that the licensee had on
-
                      two' occasions failed to promptly report a Notice of Unusual Event
During a full' participation exercise, the licensee demonstrated
                      (NOVE) and also failed to recognize an explosion as requiring entry
:
                      into the emergency classification logic during the emergency                                                                                           j
'
                      exercise.
that they could satisfactorily respond to an emergency at the
                      In the security area, a high number of hardware equipment inade-
facility.
                      quacies exist. These inadequacies, which are a result of the
However, weaknesses were noted in that the licensee had on
                      security equipment being obsolete, have lead to a continuous depen-
two' occasions failed to promptly report a Notice of Unusual Event
                      dence on compensatory measures.                             Corporate support was weak because
(NOVE) and also failed to recognize an explosion as requiring entry
                      of a high turnover rate; however, the licensee has finalized a
into the emergency classification logic during the emergency
                      reorganization of its Corporate Nuclear Security Service Branch which
j
                      has resulted in some improvements. The site management has been
exercise.
                      instrumental in dedicating site support to help the security branch
In the security area, a high number of hardware equipment inade-
                      reduce the number of security compensatory measures.
quacies exist.
                      The Engineering / Technical Support ac'tivities did not significantly                                                                                 i
These inadequacies, which are a result of the
                      exceed minimum regulatory requirements.                               While numerous issues were
security equipment being obsolete, have lead to a continuous depen-
                      resolved - during the assessment period, many of the issues were                                                                                     ;
dence on compensatory measures.
                      resolved only after considerable NRC input. Support for operations                                                                                   I
Corporate support was weak because
                      of the plant was initially viewed as a weakness but improved late in
of a high turnover rate; however, the licensee has finalized a
                      the assessment period.
reorganization of its Corporate Nuclear Security Service Branch which
                                                                                                                                                                            4 ~
has resulted in some improvements.
                      In .the Safety Assessment / Quality Verification area, the most
The site management has been
                      important improvement was in the corrective action program which made
instrumental in dedicating site support to help the security branch
          .          significant strides during the assessment period. Strengths included
reduce the number of security compensatory measures.
                      the significant management attention to and involvement in the
The Engineering / Technical Support ac'tivities did not significantly
                      corrective action process, the strong leadership provided by the
i
                      plant manager and new site director in getting employees to accept                                                                                   'j
exceed minimum regulatory requirements.
                                                                                                                                                                            '
While numerous issues were
                      responsibility for doing quality work, the quality monitoring and
resolved - during the assessment period, many of the issues were
                      audit program, and the employee concerns program. Weaknesses in-
;
                      cluded the 10 CFR 50.59 safety evaluation program and the slipping of
resolved only after considerable NRC input.
                      the dates and scope changes for commitments made to the NRC.                                                                                         3
Support for operations
            C.       Overview
I
                      February 4,1988 - February 3,1989
of the plant was initially viewed as a weakness but improved late in
                      Functional Area                                               Rating                                     Trend                                       ,
the assessment period.
                      Plant Operations.................... 2                                                                   None
4
                      Radiological Controls............... 2                                                                   None
In .the Safety Assessment / Quality Verification area, the most
                      Maintenance / Surveillance............ 2                                                           .None
~
                      Emergency Preparedness.............. 2                                                                   None
important improvement was in the corrective action program which made
                      Security............................ 2                                                                   None
significant strides during the assessment period.
                      Engineering / Technical Support....... 3                                                                   Improving
Strengths included
                      Safety Assessment /                                                                                                                                   '
.
                        Quality Veri fica ti on. . . . . . . . . . . . . . 2                                                   None
the significant management attention to and involvement in the
                                              -   _         _     - - _ _ _ _ _ _ .         _ . . . _ - - - _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ -
corrective action process, the strong leadership provided by the
' j
plant manager and new site director in getting employees to accept
'
responsibility for doing quality work, the quality monitoring and
audit program, and the employee concerns program.
Weaknesses in-
cluded the 10 CFR 50.59 safety evaluation program and the slipping of
the dates and scope changes for commitments made to the NRC.
3
C.
Overview
February 4,1988 - February 3,1989
Functional Area
Rating
Trend
,
Plant Operations....................
2
None
Radiological
Controls...............
2
None
Maintenance / Surveillance............ 2
.None
Emergency Preparedness.............. 2
None
Security............................
2
None
Engineering / Technical Support....... 3
Improving
Safety Assessment /
'
Quality Veri fica ti on. . . . . . . . . . . . . . 2
None
-
_
_
- - _ _ _ _ _ _ .
_ . . .
_ - - - _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ -


  - - - -     . , . , - - , , - . .
- - - -
                                            -               __
. , . , - - , , - .
            '
-
  ..t
__
          .
.
  -
'
                                                                      19
..t
            III. CRITERIA
.
                                  Licensee performance is assessed in selected functional areas, depending
19
                                  on whether the facility is in a construction or operational phase.
-
                                  Functional areas normally represent areas significant to nuclear safety
III. CRITERIA
                                  and the environment.     Some functional areas may not be assessed because of
Licensee performance is assessed in selected functional areas, depending
                                  little or no licensee activities or lack of meaningful observations.
on whether the facility is in a construction or operational phase.
                                  Special areas may be added to highlight significant observations.
Functional areas normally represent areas significant to nuclear safety
                                  The following evaluation criteria were used, as applicable, to assess each
and the environment.
                                  functional area:
Some functional areas may not be assessed because of
                                  1.     Assurance of quality, including management involvement and control;
little or no licensee activities or lack of meaningful observations.
                                  2.     Approach to the resolution of technical issues from a safety
Special areas may be added to highlight significant observations.
                                        standpoint;
The following evaluation criteria were used, as applicable, to assess each
                                  3.     Responsiveness to NRC initiatives;
functional area:
                                  4.     Enforcement history;
1.
                                  5.     Operational and construction events (including response to, analyses
Assurance of quality, including management involvement and control;
                                        of, reporting of, and corrective actions for);
2.
  .                              6.     Staffing (including management); and
Approach to the resolution of technical issues from a safety
                                  7.     Effectiveness of the training and qualification program.
standpoint;
                                  Nowever, the NRC is not limited to these criteria and others may have been
3.
                                  used where appropriate.
Responsiveness to NRC initiatives;
                                  On the basis ~ of the NRC assessment, each functional area evaluated is
4.
                                    rated according to three performance categories. The definitions of these
Enforcement history;
                                    performance categories are as follows:
5.
                                    1.   Category 1.     Licensee management attention and involvenient are
Operational and construction events (including response to, analyses
                                        readily evident and place emphasis on superior performance of nuclear
of, reporting of, and corrective actions for);
                                        safety or safeguards activities, with the resulting performance
6.
Staffing (including management); and
.
7.
Effectiveness of the training and qualification program.
Nowever, the NRC is not limited to these criteria and others may have been
used where appropriate.
On the basis ~ of the NRC assessment, each functional area evaluated is
rated according to three performance categories.
The definitions of these
performance categories are as follows:
1.
Category 1.
Licensee management attention and involvenient are
readily evident and place emphasis on superior performance of nuclear
,
safety or safeguards activities, with the resulting performance
i
substantially exceeding regulatory requirements.
Licensee resources
are ample and. effectively used so that a high level of plant and
i
personnel performance is being achieved.
Reduced NRC attention may
l
be appropriate.
2.
Category 2.
Licensee management attention to and involvement i r.
the performance of nuclear safety or safeguards activities is good.
The licensee has attained a level of performance above that needed to
,
,
i                                        substantially exceeding regulatory requirements.    Licensee resources
meet regulatory requirements.
                                        are ample and. effectively used so that a high level of plant and      i
Licensee resources are adequate and
                                        personnel performance is being achieved.    Reduced NRC attention may  l
j
                                        be appropriate.
reasonably allocated so that good plant and personnel performance is
                                    2.  Category 2.      Licensee management attention to and involvement i r.
1
                                        the performance of nuclear safety or safeguards activities is good.
being achieved.
                                        The licensee has attained a level of performance above that needed to    ,
NRC attention may be maintained at normal levels.
                                        meet regulatory requirements. Licensee resources are adequate and       j
l
                                        reasonably allocated so that good plant and personnel performance is   1
                                        being achieved. NRC attention may be maintained at normal levels.
                                                                                                                  l


-_ __                             --
-_ __
        .
--
                    *
*
          4
.
      "
4
                                                                          20
"
                                      3.   Category 3.       Licensee management attention to and involvement in
20
                                          the performance of nuclear safety or safeguards activities are not
3.
                                          sufficient. The licensee's performance does not significantly exceed
Category 3.
                                          that needed to meet minimal regulatory requirements. Licensee
Licensee management attention to and involvement in
                                          resources appear to be strained or not effectively used. NRC atten-
the performance of nuclear safety or safeguards activities are not
                                          tion should be increased above normal levels.
sufficient.
                                      The SALP Board may also include an appraisal of the performance trend
The licensee's performance does not significantly exceed
                                      of a functional area. This performance trend will only be used when
that needed to meet minimal regulatory requirements.
                                      both a definite ' trend of performance within the evaluation period is
Licensee
                                      discernable and the Board believes that continuation- of the trend may
resources appear to be strained or not effectively used.
                                      result in a change of performance level. The trend, if used, is defined
NRC atten-
                                      as:
tion should be increased above normal levels.
                                            Improving: Licensee performance was determined to be improving near
The SALP Board may also include an appraisal of the performance trend
                                            the close of the assessment period.
of a functional area.
                                            Declining: Licensee performance was determined to be declining near
This performance trend will only be used when
                                            the close of the assessment period and the licensee had not taken
both a definite ' trend of performance within the evaluation period is
                                          meaningful steps to address this pattern.
discernable and the Board believes that continuation- of the trend may
                                                                                                                    1
result in a change of performance level.
                      IV.           PERFORMANCE ANALYSIS
The trend, if used, is defined
                                      A.   Plant Operations
as:
                                            1.   Analysis                                   .
Improving: Licensee performance was determined to be improving near
                                                  The quality of operations at Sequoyah improved during the SALP
the close of the assessment period.
                                                  assessment period based on the results of routine and special
Declining: Licensee performance was determined to be declining near
                                                  inspections. During the first half of the assessment period,
the close of the assessment period and the licensee had not taken
                                                  several plant -trips and operational events occurred which
meaningful steps to address this pattern.
                                                  demonstrated that the operations area required further improve-
1
                                                  ment.   Following an NRC/TVA management meeting to discuss the
IV.
                                                  root causes of the poor performance which caused the trips, the   i
PERFORMANCE ANALYSIS
                                                  Sequoyah plant staff exhibited increased responsiveness to NRC   l
A.
                                                  issues, attention to detail, and commitment to quality.
Plant Operations
                                                                                                                    '
1.
                                                  Increased management attention to and involvement in the opera-
Analysis
                                                  tion of the plant contributed to a Unit 2 record power run
.
                                                  following the management conference.     Management initiatives
The quality of operations at Sequoyah improved during the SALP
                                                  included revisions to the root cause assessment procedures,
assessment period based on the results of routine and special
                                                  establishment of a requirement for PORC approval of post trip
inspections.
                                                  reviews prior to restart, increased attention to control of
During the first half of the assessment period,
                                                  plant activities, and a conscientious effort to reduce the
several plant -trips and operational events occurred which
                                                  number of inoperable or out of service components.
demonstrated that the operations area required further improve-
                                                                                                                    i
ment.
                                                  Management attention to and involvement in the upgrading of
Following an NRC/TVA management meeting to discuss the
                                                . operating procedures were focused both by results from NRC       !
root causes of the poor performance which caused the trips, the
                                                  inspections, which occurred near the end of the basis period and ,
i
                                                  during the assessment period, and by licensee initiatives.       l
Sequoyah plant staff exhibited increased responsiveness to NRC
                                                  Operating procedures were included in the licensee's ongoing
l
                                                  procedure enhancement program.     Standardizing the procedure
'
                                                                                                                  .
issues, attention to detail, and commitment to quality.
km         ____m-.___ _ _ _ _ _ _
Increased management attention to and involvement in the opera-
tion of the plant contributed to a Unit 2 record power run
following the management conference.
Management initiatives
included revisions to the root cause assessment procedures,
establishment of a requirement for PORC approval of post trip
reviews prior to restart, increased attention to control of
plant activities, and a conscientious effort to reduce the
number of inoperable or out of service components.
i
Management attention to and involvement in the upgrading of
. operating procedures were focused both by results from NRC
!
inspections, which occurred near the end of the basis period and
,
l
during the assessment period, and by licensee initiatives.
Operating procedures were included in the licensee's ongoing
procedure enhancement program.
Standardizing the procedure
.
km
____m-.___ _ _ _ _ _ _


                                                                                      __   - _ _ _ - _ _ -
__
        *
- _ _ _ - _ _ -
    .
*
                                                                                                            '
.
      .:
'
  *
.:
*
21
'
'
                                                  21
,
                                                                    ,
format and clarifying instruction steps as part of the
                          format and clarifying instruction steps as part of the
enhancement program were elements of the program initiated
                          enhancement program were elements of the program initiated
during the latter part of the assessment period.
                          during the latter part of the assessment period.     This is a
This is a
                          long-term program and is not expected to be complete during the
long-term program and is not expected to be complete during the
                          next SALP rating period. System Operating Instruction (S01)
next SALP rating period.
                          checklists were reviewed and revised by the licensee after NRC
System Operating Instruction (S01)
                          inspections during the basis period revealed prcblems with the
checklists were reviewed and revised by the licensee after NRC
                          system alignment processes. After the licensee completed these
inspections during the basis period revealed prcblems with the
                          revisions, system operating instructions were workable and
system alignment processes.
                          adequate. However, the procedure change process was difficult
After the licensee completed these
                          and cumbersome. The use of night orders to circumvent the need
revisions, system operating instructions were workable and
                          to revise operating procedures was stopped. TS' interpretations
adequate.
                          were upgraded and now require specific approval prior to their
However, the procedure change process was difficult
                          entry into the TS Interpretations log. The Emergency Operating
and cumbersome.
                          Procedures (EOPs) were determined to be adequate and the
The use of night orders to circumvent the need
                          corrective actions initiated by the licensee from a basis period
to revise operating procedures was stopped.
                          inspection were determined to be appropriate.         The
TS' interpretations
                          Administrative Instruction for controlling Hold Orders was
were upgraded and now require specific approval prior to their
                          revised to require more control by the Operations staff and more
entry into the TS Interpretations log.
                          responsibility by the persons performing the work resulting in
The Emergency Operating
                          an improved hold order process. Upgrading cf the system logic                   ;
Procedures (EOPs) were determined to be adequate and the
                          drawings for those systems. described by the Design Baseline and               ;
corrective actions initiated by the licensee from a basis period
                          Verification Program (DBVP) boundary was completed during the
inspection were determined to be appropriate.
                          assessment period and the drawings were returned to the control
The
                          room for use by the operators. Also, drawings essential for
Administrative Instruction for controlling Hold Orders was
                          safe plant operations were available in the control room. At
revised to require more control by the Operations staff and more
                          the end of the assessment period, a lcrg-term effort was in
responsibility by the persons performing the work resulting in
                          progress to restore other system logics to the prinary drawirg
an improved hold order process.
                          list and return them to the control room.
Upgrading cf the system logic
                          The licensee's approach to the resolution of technical issues
;
                          from an operational safety standpoint was technically sound. An
drawings for those systems. described by the Design Baseline and
                          understanding of the safety aspects was apparent, and censerva-
;
                          tism was usually exhibited when responding to scfety-significant
Verification Program (DBVP) boundary was completed during the
                          events and issues. Notable exceptions to this generalization
assessment period and the drawings were returned to the control
                          were the poor planning and management ineffectiveness in dealing
room for use by the operators.
                          with the system alignment and operability determination in
Also, drawings essential for
                          support of UHI valve repair, and in the resin transfer opera-
safe plant operations were available in the control room.
                          tions which occurred near the end of the assessment period.
At
                          Several operational plant events that occurred during the
the end of the assessment period, a lcrg-term effort was in
                            restart of both Units 2 and 1-identified that a poor feedwater
progress to restore other system logics to the prinary drawirg
                          control system design and operating philosophy existed.   Changes
list and return them to the control room.
                            to procedures and specifi'c operator training to eliminate trips
The licensee's approach to the resolution of technical issues
                            and transients in this area were not initially effective. Rect
from an operational safety standpoint was technically sound. An
                            cause determinations did not involve sufficient first line
understanding of the safety aspects was apparent, and censerva-
                          operations management efforts which resulted in a protracted
tism was usually exhibited when responding to scfety-significant
                            resolution process.
events and issues.
                            Improvements in the area of communications were instituted
Notable exceptions to this generalization
                            following an incident involving manipulation of the wrong valve
were the poor planning and management ineffectiveness in dealing
                            by an auxiliary unit operator which resulted in a loss of RHR
with the system alignment and operability determination in
                            suction. Control room professionalism was adequate and showed
support of UHI valve repair, and in the resin transfer opera-
        _ - _________-_ _
tions which occurred near the end of the assessment period.
Several operational plant events that occurred during the
restart of both Units 2 and 1-identified that a poor feedwater
control system design and operating philosophy existed.
Changes
to procedures and specifi'c operator training to eliminate trips
and transients in this area were not initially effective. Rect
cause determinations did not involve sufficient first line
operations management efforts which resulted in a protracted
resolution process.
Improvements in the area of communications were instituted
following an incident involving manipulation of the wrong valve
by an auxiliary unit operator which resulted in a loss of RHR
suction.
Control room professionalism was adequate and showed
_ - _________-_ _


  .                                                                       _ _ - _ _ __--
.
          '
_ _ - _ _ __--
      *
'
*
1,,
1,,
        .
.
    *
*
                                          22
22
              continued improvement during the assessment period. The
continued improvement during the assessment period.
              control room was upgraded through extensive cosmetic
The
              improvements such as new carpeting, painting, and repair of
control
              deficiencies such as roof leaks.       However, several functional
room was upgraded through extensive cosmetic
              deficiencies exist which affect operator performance and
improvements such as new carpeting, painting, and repair of
              effectiveness. Nuisance alarms, long-sta.nding hold orders and
deficiencies such as roof leaks.
              Temporary Alterations (TACFs), and human factors problems
However, several functional
              associated with steam generator level controls continued to
deficiencies exist which affect operator performance and
              cause an unwarranted number of problems for the operators.
effectiveness.
              Management was aware of these problems and is addressing them in
Nuisance alarms, long-sta.nding hold orders and
              the form of a System Engineering concept and a detailed control
Temporary Alterations (TACFs), and human factors problems
              room design review.
associated with steam generator level controls continued to
              Problems continued in the configuration control area (system
cause an unwarranted number of problems for the operators.
              alignment) through the startup of Unit 2 particularly in the
Management was aware of these problems and is addressing them in
              area of waste water systems.       The program for controlling the
the form of a System Engineering concept and a detailed control
              configuration and operations of the waste water systems was
room design review.
              changed to provide the same level of control for these systems
Problems continued in the configuration control area (system
              as was. applied to other plant systems that are under the
alignment) through the startup of Unit 2 particularly in the
            ., authority of operations.       This proved to be a positive step in
area of waste water systems.
              reducing configuration control errors associated with the waste
The program for controlling the
              water systems.     Additional changes made in the configuration
configuration and operations of the waste water systems was
              control program consisted of repeat back communication, and
changed to provide the same level of control for these systems
              separating the first and second verification by time and distance.
as was. applied to other plant systems that are under the
              The latter change had been previously recommended during the
authority of operations.
              basis period by the licensee's Unit 2 operational readiness
This proved to be a positive step in
              review team, but had not yet been implemented by managcment.             ;
.,
              Once implemented, these changes significantly reduced configu-           l
reducing configuration control errors associated with the waste
              ration control problems.
water systems.
              The licensee performed evaluations to confirm that compensatory
Additional changes made in the configuration
              measures which had previously been established for disabled
control program consisted of repeat back communication, and
              safety functions were properly documented and were collectively
separating the first and second verification by time and distance.
              and individually capable of being performed with normal staffing
The latter change had been previously recommended during the
                levels. Operator awareness and control of long standing TACFs
basis period by the licensee's Unit 2 operational readiness
                in relation to their effect on plant configuration was a matter
review team, but had not yet been implemented by managcment.
              of concern to the NRC during the basis period and continued to
;
              be an issue during the assessment period. The licensee took
Once implemented, these changes significantly reduced configu-
              action to reduce the number of TACFs to approximately 80, which
l
              was 50% of the level at the beginning of the period, with a goal
ration control problems.
              of having no more than approximately 30 TACFs.
The licensee performed evaluations to confirm that compensatory
              Operators were well informed in the use of emergency operating
measures which had previously been established for disabled
                procedures.   Because of the long duration shutdown period
safety functions were properly documented and were collectively
                (approximately 21 years), the number of reactor operators
and individually capable of being performed with normal staffing
              experienced in power operations was low and additional support
levels.
                personnel were made available in preparation for Unit 2 restart.
Operator awareness and control of long standing TACFs
              These included additional management presence in the control
in relation to their effect on plant configuration was a matter
                room, additional control room Senior Reactor Operators, and
of concern to the NRC during the basis period and continued to
                temporary Operating Shift Advisors. Operator actions for most
be an issue during the assessment period.
                events that occurred during the Unit 2 startup were appropriate.
The licensee took
.
action to reduce the number of TACFs to approximately 80, which
                                                                                        j
was 50% of the level at the beginning of the period, with a goal
                                                                                        !
of having no more than approximately 30 TACFs.
                                        ..
Operators were well informed in the use of emergency operating
procedures.
Because of the long duration shutdown period
(approximately 21 years), the number of reactor operators
experienced in power operations was low and additional support
personnel were made available in preparation for Unit 2 restart.
These included additional management presence in the control
room, additional control room Senior Reactor Operators, and
temporary Operating Shift Advisors.
Operator actions for most
events that occurred during the Unit 2 startup were appropriate.
j
.
!
..


                                                                            _-
_-
      .
.
    ,
,
    g
g
  .
.
                                  23
23
        Licensed operators responded effectively to plant transients on
Licensed operators responded effectively to plant transients on
        most occasions during Unit 1 startup     including a reactor trip
most occasions during Unit 1 startup
        of Unit'l caused by' feedwater control problems, a turbine trip
including a reactor trip
        of Unit 1, a reactor trip of Unit 1 caused by a generator
of Unit'l caused by' feedwater control problems, a turbine trip
        ground, and a lightning strike of a switchyard transfonner
of Unit 1, a reactor trip of Unit 1 caused by a generator
        during a thunderstorm.                                         .
ground, and a lightning strike of a switchyard transfonner
        Operators were observed to be disciplined professionals with
during a thunderstorm.
        adequate communication skills.   However, occasional lapses which
.
        were exemplified by one instance of inadequate action by an
Operators were observed to be disciplined professionals with
        operator during routine plant activities occurred. This example
adequate communication skills.
        involved the placement of a centrifugal charging pump in the
However, occasional lapses which
        pull to lock position which resulted in a failure to comply with a
were exemplified by one instance of inadequate action by an
        technical specification action statement,
operator during routine plant activities occurred.
        Control room activities were generally conducted in an effective
This example
        and professional manner. Formal communications were observed in
involved the placement of a centrifugal charging pump in the
        most cases. Operators were attentive, aware of plant conditions
pull to lock position which resulted in a failure to comply with a
        and responsive to changes in plant conditions. Senior plant
technical specification action statement,
        management actively supported the above operator activities and         i
Control room activities were generally conducted in an effective
        was deeply involved in the day-to-day operation of the plant.
and professional manner.
        In addition senior plant management maintained a detailed
Formal communications were observed in
        account of and tracked the status of known equipment
most cases.
        deficiencies, CAQRs, and plant parameters in daily plant
Operators were attentive, aware of plant conditions
        meetings.   Active involvement by plant management and support of
and responsive to changes in plant conditions.
        ti.e ownership concept by the operations department had a             -
Senior plant
        positive' effect on plant operations and morale. This was
management actively supported the above operator activities and
        exhibited by the absence of significant- events or operating
i
        problems during the extended power run of Unit 2. Facility
was deeply involved in the day-to-day operation of the plant.
        operations reflected improvements in planning and assignment of
In addition senior plant management maintained a detailed
        priorities during the period. The forced outage rate for both
account
        units during the period was extremely high as a result of the
of
        extended shutdown. However, following the five Unit 2 trips
and
        which occurred early in the Unit 2 startup process, Unit 2 had
tracked
        no forced outages for a period of approximately 210 days.
the status of known equipment
        Unit 1 experienced two reactor trips during its startup period,
deficiencies, CAQRs, and plant parameters in daily plant
        followed by full availability for the remainder of the
meetings.
        assessment period.
Active involvement by plant management and support of
        Management support and insistence on the ownership concept has
ti.e ownership concept by the operations department had a
        strengthened the authority and role of the Operations group in
-
        general and the control room shift supervisor in particular.
positive' effect on plant operations and morale.
        Operations personnel have demonstrated on many occasions their
This was
        willingness to suspend or delay surveillance, maintenance ard
exhibited by the absence of significant- events or operating
        other schedule impacting activities until they were satisfied
problems during the extended power run of Unit 2.
          that the plant was in a safe stable condition and that other
Facility
          plant activities in progress would not interact with the
operations reflected improvements in planning and assignment of
          scheduled activities to produce safety system actuations. The
priorities during the period.
          absolute authority of the operations staff in these matters has
The forced outage rate for both
          been fully supported by plant management.
units during the period was extremely high as a result of the
extended shutdown.
However, following the five Unit 2 trips
which occurred early in the Unit 2 startup process, Unit 2 had
no forced outages for a period of approximately 210 days.
Unit 1 experienced two reactor trips during its startup period,
followed by full availability for the remainder of the
assessment period.
Management support and insistence on the ownership concept has
strengthened the authority and role of the Operations group in
general and the control room shift supervisor in particular.
Operations personnel have demonstrated on many occasions their
willingness to suspend or delay surveillance, maintenance ard
other schedule impacting activities until they were satisfied
that the plant was in a safe stable condition and that other
plant activities in progress would not interact with the
scheduled activities to produce safety system actuations. The
absolute authority of the operations staff in these matters has
been fully supported by plant management.
l-
l-
                                                                                i
L
L
i


  - _ _ - _ .
- _ _ - _ .
                      ,
,
              *
*
  .
.
    .
.
-
-
                                          24
24
                During the assessment period the licensee administered             i
During the assessment period the licensee administered
                requalification examinations. The results from the examinations
i
                indicated a large percentage success rate (approximately 69 cut
requalification examinations.
                of 70).     Nonlicensed operators were judged to be extensively
The results from the examinations
                trained receiving both detailed classroom training and thorough   {
indicated a large percentage success rate (approximately 69 cut
                                                                                    "
of 70).
                in plant on the job training.     The percentage success rate for
Nonlicensed operators were judged to be extensively
                new operating license candidates was determined to be
trained receiving both detailed classroom training and thorough
                below average (7 out of 11 passed).
{
                Operations shift training for newly installed plant modifica-     ,
in plant on the job training.
                tions and for correction of operating deficiencies or events was   i
The percentage success rate for
                adequate.- However, occasional lapses were exemplif.ied by the
"
                shutdown margin / excessive cooldown events and rod control demand
new operating license candidates was determined to be
                counter problems.
below average (7 out of 11 passed).
                During the assessment period Operating shift manning was           l
Operations shift training for newly installed plant modifica-
                adequate and maintained at the levels established during the
,
                basis period. Several management positions were eliminated to
tions and for correction of operating deficiencies or events was
                streamline the Operations organization which resulted in a more
i
                effective organization.
adequate.- However, occasional lapses were exemplif.ied by the
                Management stressed procedural compliance by operations per-
shutdown margin / excessive cooldown events and rod control demand
                sonnel throughout the assessment period. This had a side effect
counter problems.
                of improving procedures by forcing operators to have inadequate
During the assessment period Operating shift manning was
                procedures revised before they could be used.         However,
l
                instances of procedural non-compliance and deviation continued
adequate and maintained at the levels established during the
                during Unit 2 startup, such as the MSIV closures, configuration
basis period.
                control deviations, and Upper Head Injection (UHI) accumu'lator
Several management positions were eliminated to
                venting events. Management was very aggressive in responding to
streamline the Operations organization which resulted in a more
                the above issues and by the middle of the assessment period
effective organization.
                procedural adherence was adequate and improving.
Management stressed procedural compliance by operations per-
                  In an event involving the discharge of highly-radioactive spent
sonnel throughout the assessment period.
                  resin that occurred during the lctter portion of the SALP
This had a side effect
                assessment period, it was determined that the intense management
of improving procedures by forcing operators to have inadequate
                attention given to power operations had not been applied to the
procedures revised before they could be used.
                waste processing portion of the power plant and the attendant
However,
                  operations support staff. This event highlighted, in that area
instances of procedural non-compliance and deviation continued
                  alerte, inadequate procedures, a casual attitude toward following
during Unit 2 startup, such as the MSIV closures, configuration
                  procedures, inadequate drawing control, and failure to aggres-
control deviations, and Upper Head Injection (UHI) accumu'lator
                  sively correct design problems that make cperations awkward or
venting events.
                  could create personnel or radiological hazards. In addition,
Management was very aggressive in responding to
                  plant management in this specific area appeared to be poorly
the above issues and by the middle of the assessment period
                  trained and very weak with respect to the operating and physical
procedural adherence was adequate and improving.
                  characteristics of their assigned system.   Finally, interactions
In an event involving the discharge of highly-radioactive spent
                  between the waste and water management group and other plant
resin that occurred during the lctter portion of the SALP
                management that were observed following this event did not
assessment period, it was determined that the intense management
                  demonstrate a cooperative, quality-oriented approach to the
attention given to power operations had not been applied to the
                  resolution of technical issues within the waste and water
waste processing portion of the power plant and the attendant
                  management group.   Plant management is currently taking strong
operations support staff.
                  corrective action to improve the waste water processing area.
This event highlighted, in that area
      _-
alerte, inadequate procedures, a casual attitude toward following
procedures, inadequate drawing control, and failure to aggres-
sively correct design problems that make cperations awkward or
could create personnel or radiological hazards. In addition,
plant management in this specific area appeared to be
poorly
trained and very weak with respect to the operating and physical
characteristics of their assigned system.
Finally, interactions
between the waste and water management group and other plant
management that were observed following this event did not
demonstrate a cooperative, quality-oriented approach to the
resolution of technical issues within the waste and water
management group.
Plant management is currently taking strong
corrective action to improve the waste water processing area.
_-


    _                                   _   _.
_
p     ,
_
                          r
_.
p
r
,
L
<
'
25
L
L
        <
Logkeeping by licensed operators continued to exhibit weaknesses
    '                                                                  25
particularly -in the areas of detailed entries, entry and exit
L                                              Logkeeping by licensed operators continued to exhibit weaknesses
from Limiting Condition for Operation (LCOs), and descriptive
                                              particularly -in the areas of detailed entries, entry and exit
explanations and rationales for decisions made and actions
                                              from Limiting Condition for Operation (LCOs), and descriptive
conducted by the operators and SR0s.
                                              explanations and rationales for decisions made and actions
During the last' two moriths-
                                              conducted by the operators and SR0s. During the last' two moriths- l
l
                                                                                                                  '
of the assessment period, Operations management implemented
                                              of the assessment period, Operations management implemented
'
                                              corrective actions in these areas by having' Operations super-
corrective actions in these areas by having' Operations super-
                                              visors review logs for completeness, stand-alone entries and
visors review logs for completeness, stand-alone entries and
                                              supportable explanations for LC0 entries, exits and changes to
supportable explanations for LC0 entries, exits and changes to
                                              plant and equipment status. The NRC identified during the
plant and equipment status.
                                              latter portion of the assessment period a significant
The NRC identified during the
                                              improvement in the level of detail supporting log entries.     The
latter portion of the assessment period a significant
                                              corrective actions were effective.
improvement in the level of detail supporting log entries.
                                              Operational events in general were promptly and accurately
The
                                          '
corrective actions were effective.
                                              identified. Exceptions were the failure of the operations staff
Operational events in general were promptly and accurately
                                              to recognize problems with the excessive post-trip cooldowns,
identified.
                                              and having a centrifugal charging pump in pull-to-lock while the
Exceptions were the failure of the operations staff
                                              other pump was inoperable, both of which resulted in escalated
'
                                              enforcement.
to recognize problems with the excessive post-trip cooldowns,
                                              Emergency Notification System (ENS) reports occurred at a high
and having a centrifugal charging pump in pull-to-lock while the
                                              rate as a result of the special outage conditions and system
other pump was inoperable, both of which resulted in escalated
                                              configurations. Notifications were generally conservatively
enforcement.
                                              made 'and technically correct. ENS notification was not made
Emergency Notification System (ENS) reports occurred at a high
                                      -
rate as a result of the special outage conditions and system
                                              initi, ally for the centrifugal charging purp in pull-to-lock
configurations.
                                              event,. and for an unidentified RCS leakage above allowable
Notifications were generally conservatively
  '
made 'and technically correct.
                                              incident. DNE support of Operations in making Operability
ENS notification was not made
                                              determinations improved during the assessn.ent period. This
initi, ally for the centrifugal charging purp in pull-to-lock
                                              improvement was the result of management initiatives and
-
                                              personnel changes.
event,. and for an unidentified RCS leakage above allowable
                                              As a result of the change in licensee management that occurred
incident.
                                              at the'end of the basis period, PORC reviews became aggressive
DNE support of Operations in making Operability
                                              and technically involved in the resolution of issues affecting
'
                                              the safe operation of the unit.     Changes in PORC activities
determinations improved during the assessn.ent period.
                                              which resulted in improved performance included consistency in
This
                                              personnel staffing and the high expectations established by the
improvement was the result of management initiatives and
                                              new plant manager. The elevated expectations were also strongly
personnel changes.
                                              supported by the new site director and upper TVA management. As
As a result of the change in licensee management that occurred
                                              a result of the TVA management initiatives, the Plant Operations
at the'end of the basis period, PORC reviews became aggressive
                                              Review Staff was established as a part time support group for
and technically involved in the resolution of issues affecting
                                              PORC.   P0RS employed specialized training and skills to perform
the safe operation of the unit.
                                                root cause evaluations and determine corrective action plans
Changes in PORC activities
                                              associated with plant events, which were then submitted cs
which resulted in improved performance included consistency in
                                              completed projects to PORC. The use of the Plant Operations
personnel staffing and the high expectations established by the
                                              Review Staff has involved the PORC deeply in day-to-day plant
new plant manager.
                                              operations.
The elevated expectations were also strongly
                                                                                                                  i
supported by the new site director and upper TVA management. As
          - _ _ - - - _ _ _ . _ _ _ .
a result of the TVA management initiatives, the Plant Operations
Review Staff was established as a part time support group for
PORC.
P0RS employed specialized training and skills to perform
root cause evaluations and determine corrective action plans
associated with plant events, which were then submitted cs
completed projects to PORC.
The use of the Plant Operations
Review Staff has involved the PORC deeply in day-to-day plant
operations.
i
- _ _ - - - _ _ _ . _ _ _ .


              ,                                                                               . _ _ _ _
,
              yq>   + t
. _ _ _ _
    ,
+ t
        .
yq>
    g.A
,
          '
.
                  ,
g.A
                                                      26    ,
'
                                                                                                        l
26
w
l
[                        eat the close of the:SALP assessment period Sequoyah upper line
,
                                    ~
,
        '
w[
eat the close of the:SALP assessment period Sequoyah upper line
'
~
management was found to .be strongly comnitted to obtaining
;
"
quality'in plant operations. .There was also a general increase-
.
.in management attention toward the ccnduct of operations and-
l
. management awareness of plant conditions.
These, coupled with
!
organizational changes to reduce both. management resistance to
i
change; and the number of management levels, resulted in _ _
l
continuing improvement'in the performance of the operating staff
l
'
-
and the resolution of technically diverse and complex issues
!
$
throughout the year.
;
p
i,
During this assessment period the entire fire protection staff
;
at Sequoyah was reorganized into a Fire Operaticns Unit.
The
l
Fire Operations Unit consists of a dedicated fire brigade which
:
'is responsible for fire suppression and fire prevention
,
inactivities.
The dedicated fire brigade replaced the preexisting
]
system of_ a fire brigede composed of unit operations personnel.
1
Fire: brigade' training at TVA's Nickajack Fire Training Center
j
was fourd to be excellent and brigade manning was determined to
i
be adequate.
Reorganization of the fire protection staff
j
. greatly improved fire brigade effectiveness and fire prevention
!
activities during this assessment period. Organizational
i
planning and assignment of- priorities was demonstrated in the
l
fire ' brigade reorganization.
In general, policies and pro-
,
cedures were well stated and understood.
~Under the reorganized
!
'
fire operations unit, decision making was usually at a level
!
that ensured adequate management review.
Involvement by
"
"
                            management was found to .be strongly comnitted to obtaining                  ;
;
                            quality'in plant operations. .There was also a general increase-            .
corporate management in the fire protection area was evident.
                        .in management attention toward the ccnduct of operations and-                  l
Two . Fire' Protection QA Audits were performed during the SALP
                        . management awareness of plant conditions. These, coupled with                 !
j
                            organizational changes to reduce both. management resistance to              i
i
                            change; and the number of management levels, resulted in _ _                l
'
            '
assessment period, one of which was by the licensee's insurer,
                            continuing improvement'in the performance of the operating staff            l
. American , Nuclear Insurers ( ANI).
      -
These audits icentified a
                            and the resolution of technically diverse and complex issues                !
i
      $                    throughout the year.                                                         ;
number of unsatisfactory conditions and findings and reccarended
p        i,                 During this assessment period the entire fire protection staff              ;
i
                            at Sequoyah was reorganized into a Fire Operaticns Unit. The                l
several program improvements.
                            Fire Operations Unit consists of a dedicated fire brigade which              :
The licensee either implemented
                        'is responsible for fire suppression and fire prevention                        ,
i
                        inactivities.    The dedicated fire brigade replaced the preexisting          ]
E
                            system of_ a fire brigede composed of unit operations personnel.             1
the - corrective actions associated with these findings or
                            Fire: brigade' training at TVA's Nickajack Fire Training Center              j
evaluatcd the issues to develop a schedule date for completion
                            was fourd to be excellent and brigade manning was determined to             i
;
                            be adequate.     Reorganization of the fire protection staff                j
of the corrective' actions.
                          . greatly improved fire brigade effectiveness and fire prevention              !
The NRC identified weaknesses
                            activities during this assessment period. Organizational                    i
in
                            planning and assignment of- priorities was demonstrated in the              l
~
                            fire ' brigade reorganization. In general, policies and pro-                 ,
the areas of procedural implementation of fire penetration
                                                                        ~Under the reorganized
,
                          '
barrier requirements and control of combustibles. The new fire
                            cedures were well stated and understood.                                     !
i
                            fire operations unit, decision making was usually at a level                !
protection management was aggressive in the resolution of these
"                          that ensured adequate management review.        Involvement by              ;
i
                            corporate management in the fire protection area was evident.
issues and appeared to take appropriate corrective actions.
                            Two . Fire' Protection QA Audits were performed during the SALP              j
!
                                                                                                        i
!
. The condition of Fire 4arriers, surveillance of fire protection
l
^
syst' ems and components, emergency lighting, manual equipment and
l
QA audits were satisfactory in terms of the low number of
l
deficiencies noted.
Housekeeping practices and conditions
;
relative to fire. protection wera found to be adequate.
l
l
During the SALP assessment period inadequacies in the perfor-
mance of fire watches were noted.
The inadequacies consisted of
;
inadequate inanagement oversight in regar d to fire watch per-
:
l
y
.
!
 
,
___
.
'
'
                            assessment period, one of which was by the licensee's insurer,
e
                          . American , Nuclear Insurers ( ANI).  These audits icentified a              i
6
                            number of unsatisfactory conditions and findings and reccarended            i
27
                            several program improvements. The licensee either implemented                i
-
E                          the - corrective actions associated with these findings or
sonnel and failure. of management to provide concise guidance on
                            evaluatcd the issues to develop a schedule date for completion              ;
how fire watch individuals must perform their duties.
                            of the corrective' actions. The NRC identified weaknesses in
This
                                                                                                        ~
issue occurred at the time that the new organization was being
                            the areas of procedural implementation of fire penetration                  ,
put into place and was aggressively pursued by the new fire
                            barrier requirements and control of combustibles. The new fire              i
organization management.
                            protection management was aggressive in the resolution of these              i
Five violations and one deviation were identified:
                            issues and appeared to take appropriate corrective actions.                 !
j
                                                                                                        !
a.
  ^
Severity Level III violation for failure to comply with TS
                          . The condition of Fire 4arriers, surveillance of fire protection              l
!
                            syst' ems and components, emergency lighting, manual equipment and          l
3.0.3 involving loss of safety functions and for failure to
                            QA audits were satisfactory in terms of the low number of                    l
notify the NRC in a timely manner. (88-20-03 & 88-20-04)
                            deficiencies noted. Housekeeping practices and conditions                    ;
b.
                            relative to fire. protection wera found to be adequate.                      l
Severity Level IV violation for failure to implement
                                                                                                        l
configuration controls. (88-26-01)
                            During the SALP assessment period inadequacies in the perfor-
c.
                            mance of fire watches were noted. The inadequacies consisted of              ;
Severity Level IV violation for failure to meet require-
                            inadequate inanagement oversight in regar d to fire watch per-
ments of TS 3.3.1 and 3.3.2 to place OTDT and OPDT in trip.
                y
(88-39-02)
                                                                                                        :
d.-
                                                                                                        l
Severity Level IV violation for failure to perform fire
watch patrols.
(88-46-01)
e.
Severity Level IV violation for performing a test of the
TDAFW pump without a written procedure.
(88-48-02)
f.
Deviation for failure to comply with a commitment made
concerning the control of combustibles (wood) in safety-
related areas.
(88-54-01)
.
.
                                                                                                        !
2.
Performance Rating:
Category 2
3.
Recommendations:
The Board recognized that significant experience was gained
through the plant events and activities which occur ed
,
during the assessment period and resulted in an improvement
in the plant operations area.
!
B.
Radiological Controls
1.
Analysis
During the assessment period, inspections were performed by the
resident and Regional office staff in the areas of ram *+'on
protection, radiologi, cal effluent, and confirmatory meure-
ments.
Included in the inspection program was a special team
inspection for restart of Unit 1 and a special team inspection
to assess the performance of health physics, chemistry, and
radioactive waste processing during the recent outage.


,     ___
_
                                                      .
_-_---
        '
-_
  e
e
    6
,
  -                                         27
.' .
                  sonnel and failure. of management to provide concise guidance on
,
                  how fire watch individuals must perform their duties. This
'
                  issue occurred at the time that the new organization was being
28
                  put into place and was aggressively pursued by the new fire
The' qualifications of the new Superintendent of Radiological
                  organization management.
Controls posi* ion were determined to have met the requirements
                  Five violations and one deviation were identified:                j
- discussed _ in Regulatory Guide 1.8, Qualification and Training of-
                  a.    Severity Level III violation for failure to comply with TS  !
Personnel for Nuclear Power Plants.
                        3.0.3 involving loss of safety functions and for failure to
The licensee's health physics, radwaste,. and chemistry staffing
                        notify the NRC in a timely manner. (88-20-03 & 88-20-04)
levels were adequate and compared well with other utilities -
                  b.   Severity Level IV violation for failure to implement
having' facilities of'similar size.
                        configuration controls. (88-26-01)
An adequate number of ANSI
                  c.   Severity Level IV violation for failure to meet require-
qualified licensee health physics (HP) technicians were
                        ments of TS 3.3.1 and 3.3.2 to place OTDT and OPDT in trip.
available to support . routine operations.
                        (88-39-02)
During outage
                  d.-   Severity Level IV violation for failure to perform fire
operations, additional contract health physics technicians were
                        watch patrols.    (88-46-01)
used to supplement the permanent health physics staff.
                  e.   Severity Level IV violation for performing a test of the
The
                        TDAFW pump without a written procedure.   (88-48-02)
overall quality and experience level of the health physics staff
                  f.    Deviation for failure to comply with a commitment made
is-viewed as a program strength.
                        concerning the control of combustibles (wood) in safety-
Radiation protection training
                        related areas. (88-54-01)
was considered good.
                                                              .
The licensee's general employee training
                  2.    Performance Rating:
(GET) in radiation protection was well' defined.
                        Category 2
The GET
                  3.    Recommendations:
training / retraining program not only included standard topics as
                        The Board recognized that significant experience was gained
outlined in 10 CFR 19, but findings of licensee audits and NRC
                        through the plant events and activities which occur ed ,
inspections were factored into the training.
                        during the assessment period and resulted in an improvement
Management support
                        in the plant operations area.
of and commitment to training was evident in that sufficient-
              Radiological Controls                                                !
time was allowed for training and employees were encouraged to
          B.
attend.
              1.  Analysis
Management support and involvement in matters related to
                  During the assessment period, inspections were performed by the
radiation protection were demonstrated by:
                  resident and Regional office staff in the areas of ram *+'on
(1) purchasing an
                  protection, radiologi, cal effluent, and confirmatory meure-
automated laundry monitor to control the potential for " hot
                  ments.   Included in the inspection program was a special team
-
                  inspection for restart of Unit 1 and a special team inspection
particles" in order to reduce exposure to personnel;
                  to assess the performance of health physics, chemistry, and
(2) installir.g seven sensitive portal monitors at the exit to
                  radioactive waste processing during the recent outage.
the . radiation controlled area (RCA) to be more effective in
detecting personnel contaminations; (3) establishing an ALARA
incentive program; and (4) providing corporate support in
resolving technical isst'es as related to the radiation protec-
-tion program.
Resolution of technica: issues was generally adequate; however,
a special team inspection observed, during the Unit 2 refueling
outage at the end of the assessment period, that the licensee
experienced problems in containment such as high iodine airborne
radioactivity, an unexpected increase of beta radiation levels in
steam generators, and heat stress to personnel while wearing
supplieu oar noods.
These problems appeared to be caused by a
failure of licensee management to communicate and evaluate these
problems adequately.
Early identification and technical resolu-
tion of the root causes were not performed in a timely manner,
which created the need for increased radiological attention,
resources, and demand for support from the radiological controls
program.
During the assessment period, a special NRC inspection team
revievied the licensee's controls for high radiation areas and
determined tw tnese controls were generally adequate.
l
le__-________-____
_ _ _ _ _ .


_        _-_---  -_
. _-___ - _ __
              e
[~.
    ,
-
    .' .                                                            ,
.
  '
.
                                                28
29
                    The' qualifications of the new Superintendent of Radiological
i
                    Controls posi* ion were determined to have met the requirements
However, one violation was identified pertaining to two
                  - discussed _ in Regulatory Guide 1.8, Qualification and Training of-
-
                    Personnel for Nuclear Power Plants.
. Assistant Unit Operators (AU0s) who were unknowingly working in
                    The licensee's health physics, radwaste,. and chemistry staffing
;I
                      levels were adequate and compared well with other utilities -
-a high. radiation area in the Unit 1 Auxiliary 8uilding created
                    having' facilities of'similar size. An adequate number of ANSI
                    qualified licensee health physics (HP) technicians were
                    available to support . routine operations.        During outage
                    operations, additional contract health physics technicians were
                      used to supplement the permanent health physics staff. The
                      overall quality and experience level of the health physics staff
                      is-viewed as a program strength. Radiation protection training
                    was considered good. The licensee's general employee training
                      (GET) in radiation protection was well' defined. The GET
                      training / retraining program not only included standard topics as
                      outlined in 10 CFR 19, but findings of licensee audits and NRC
                      inspections were factored into the training. Management support
                      of and commitment to training was evident in that sufficient-
                      time was allowed for training and employees were encouraged to
                      attend.
                      Management support and involvement in matters related to
                      radiation protection were demonstrated by: (1) purchasing an
                      automated laundry monitor to control the potential for " hot      -
                      particles" in order to reduce exposure to personnel;
                      (2) installir.g seven sensitive portal monitors at the exit to
                      the . radiation controlled area (RCA) to be more effective in
                      detecting personnel contaminations; (3) establishing an ALARA
                      incentive program; and (4) providing corporate support in
                      resolving technical isst'es as related to the radiation protec-
                    -tion program.
                      Resolution of technica: issues was generally adequate; however,
                      a special team inspection observed, during the Unit 2 refueling
                      outage at the end of the assessment period, that the licensee
                      experienced problems in containment such as high iodine airborne
                      radioactivity, an unexpected increase of beta radiation levels in
                      steam generators, and heat stress to personnel while wearing
                      supplieu oar noods. These problems appeared to be caused by a
                      failure of licensee management to communicate and evaluate these
                      problems adequately. Early identification and technical resolu-
                      tion of the root causes were not performed in a timely manner,
                      which created the need for increased radiological attention,
                      resources, and demand for support from the radiological controls
                      program.
                      During the assessment period, a special NRC inspection team
                      revievied the licensee's controls for high radiation areas and
                      determined tw tnese controls were generally adequate.
l
l
by an inadvertent introduction of-reactor coolant and resin into
j
the CVCS demineralized resin transfer piping. The AU0s received
!
l
doses of between 400 and 500 mrem and did 'not exceed .any
administrative or NRC exposure limits. . It was determined that
;
~ the area was posted as a radiation area 'instead of 'a high
l
radiation area 'and that the workers had neither an integrating
l
dose . rate monitoring device nor an individual present with a
dose rate' monitoring device to provide radiological protection
job coverage. The licensee's immediate corrective action was to
post and lock the concerned high radiation area and to reconfirm
i
that other radiation and high radiation areas were adequatelv
controlled.
i
.
'
~The
respiratory protection
program was
reviewed by
the NRC during the assessment period and it was determined to t
the program was well defined and implemented in accordance with
appropriate regulations.
The 1987 collective radiation dose was 206 person-rem which was
I
'
approximately 56% of the national average of 368 person-rem pe'r
pressurized water reactor (PWR).
In 1988, the - station's
collective radiation dose was 382 person-rem, compared to 345
;
person-rem per unit national average, which when combined with
1
the 1986 and ~ 1987 collective radiation dose ' averaged 284
person-rem for three years.
However, since the unit has been
inoperative for an extended period
the three ~ year average is
not necessarily comparable to similar intervals for other units.
At the end of 1987, the area of the plant controlled as
radioactively
contaminated was approximately 15% of the total
area which potentially cruld become contaminated. At the end of
1988, the area contaminated was still approximately 15% and
slightly above other facilities similar in design, however, this
did not create a significant personnel exposure or personnel
contamination problem.
The licensee experienced 130 personnel contaminations in 1987.
The number of personnel contaminations in 1987 was among the
lowest in Region II.
However, in 1988, the number of personnel
l
l
e__-________-____                  _ _ _ _ _ .
contaminations increased to 409 and 155 of these were skin
l'
contaminations.
The increase in personnel contaminations was
due in part to startup activity at the plant, increasing
radiation levels and the increased detection sensitivity of the
new, more sensitive, portal monitors at the exit of the RCA.
Effluent summary data for 1985, IS86, and 1987, are contained
under Supporting Data and Summaries, Section I of this report.
These releases are consistent with the plant being shut down
from mid-1985_through 1987, and consequently no basis exists to
establish any trends during the assessment period.
_
_ _ _ _ _ _ _ _--___-_ _ ____ _ _ _ -


                                                                                          . _-___ - _ __
,
    [~.                                     -
-
      .
_
  .
_ - .
                                    29
__
                                                                                                            i
__
          However, one violation was identified pertaining to two                                        -
-
        . Assistant Unit Operators (AU0s) who were unknowingly working in                                ;I
_-_
          -a high. radiation area in the Unit 1 Auxiliary 8uilding created                                  l
_ _ -
          by an inadvertent introduction of-reactor coolant and resin into                                  j
_
          the CVCS demineralized resin transfer piping. The AU0s received                                  !
--_
          doses of between 400 and 500 mrem and did 'not exceed .any                                        l
l
          administrative or NRC exposure limits. . It was determined that                                  ;
<
        ~ the area was posted as a radiation area 'instead of 'a high                                      l
+
          radiation area 'and that the workers had neither an integrating                                  l
1: a
          dose . rate monitoring device nor an individual present with a
.
          dose rate' monitoring device to provide radiological protection
30
          job coverage. The licensee's immediate corrective action was to
~
          post and lock the concerned high radiation area and to reconfirm
During the' assessment period, the licensee's program for
          that other radiation and high radiation areas were adequatelv                                    i
l'
          controlled.                                                                                      i
packaging, shipping, and storage of icw level radioactive waste
                                                                                                            .
was - determined to be adequate.
                                                                                                            '
The licensee demonstrated good
        ~The    respiratory protection    program was                        reviewed by
w
          the NRC during the assessment period and it was determined to t
radioanalytical trend capability by' showing close agreement with
          the program was well defined and implemented in accordance with
NRC results for both beta-emitting and gamma-emitting samples.
          appropriate regulations.
However, weaknesses were identified in the radiological waste
          The 1987 collective radiation dose was 206 person-rem which was                                  I
'
                                                                                                            '
. water processing area as described in the operations section.of
          approximately 56% of the national average of 368 person-rem pe'r
this assessment.
          pressurized water reactor (PWR).             In 1988, the - station's
g
          collective radiation dose was 382 person-rem, compared to 345                                    ;
Two violations were identified:
          person-rem per unit national average, which when combined with                                    1
a.
            the 1986 and ~ 1987 collective radiation dose ' averaged 284
'Ssverity. Level IV violation for failure to adhere to or '
          person-rem for three years. However, since the unit has been
-
            inoperative for an extended period the three ~ year average is
establish' procedures for performing breathing: zcne air
            not necessarily comparable to similar intervals for other units.
samples and for exposure control during steam generator
          At the end of 1987, the area of the plant controlled as
work.
            radioactively contaminated was approximately 15% of the total
(08-31-02)
            area which potentially cruld become contaminated. At the end of
b.
            1988, the area contaminated was still approximately 15% and
Severity Level IV violation for failure to evaluate
            slightly above other facilities similar in design, however, this
the radiation hazards present in the 690 foot eleva-
            did not create a significant personnel exposure or personnel
tion Pipe Chase in the Auxiliary Buildine.
            contamination problem.
(89-05-04)
            The licensee experienced 130 personnel contaminations in 1987.
2..
            The number of personnel contaminations in 1987 was among the
Performance Rating:
            lowest in Region II. However, in 1988, the number of personnel
Category 2
l          contaminations increased to 409 and 155 of these were skin
3.
l'          contaminations. The increase in personnel contaminations was
Recommendations:
            due in part to startup activity at the plant, increasing
.
            radiation levels and the increased detection sensitivity of the
' Hone
            new, more sensitive, portal monitors at the exit of the RCA.
.
            Effluent summary data for 1985, IS86, and 1987, are contained
C.
            under Supporting Data and Summaries, Section I of this report.
Maintenance / Surveillance
            These releases are consistent with the plant being shut down
.1.
            from mid-1985_through 1987, and consequently no basis exists to
Analysis
            establish any trends during the assessment period.
During the assessment period, the technical quality of main-
                                          _   _ _ _ _ _ _ _ _--___-_ _ ____ _ _ _ -
tenance and surveillance at Sequoyah was good as a result of the
many technical and programmatic upgrades which occurred.
These
l
programs experienced substantial organizational and~ perscnnel
changes resulting in a large number of licensee initiatives.
The addition of a new maintenance superintendent at the
beginning of the assessment period . resulted in licensee
initiatives in the maintenance area which included; increasing
the use of system engineers, the use of.new vibration monitoring
equipment techniques, maintenance procedure enhancement,
extensive Motor Operated Valve Actuators (M0 VATS) testing of
primary and balance-of-plant valves, establishment of a 24 hour
Outage Manager to coordinate maintenance and triodification work,
and the organization of maintenance and modification activities
l
into train and system outages.
Management of the Maintenance
Program was very effective as demonstrated by positive trends in
industry indicatcrs such as maintenance backlog, tagging,
overtime use, CAQR and LER generation, QA document rejection,
Post Modification Testing (PMT) rejection requiring maintenance
_ _ _ _ _ _ _ _ - _ _ _ - _ _ _
- _ _ _ _ _ _ _ _ _ _ _ _ _ _ -


,              - _      _ - .             __                                   __    - _-_                                    _ _ -       _   --_
- - . __
l            <
_-
1: a            +
-_
            .
_
        ~
.
                                                                              30
.
                              During the' assessment period, the licensee's program for
-
l'                            packaging, shipping, and storage of icw level radioactive waste
.
                              was - determined to be adequate.                             The licensee demonstrated good
.
    w                        radioanalytical trend capability by' showing close agreement with
31
                              NRC results for both beta-emitting and gamma-emitting samples.
~
  '
rework, personnel contamination, industrial safety practices,
                              However, weaknesses were identified in the radiological waste
and delinquent safety-related preventive maintenance.
                            . water processing area as described in the operations section.of
Line
      g
management increased its presence in the operating and work
                              this assessment.
spaces, became more aware of plant status and technical issues
                              Two violations were identified:
and demonstrated a. commitment to the program and associated
          -                    a.  'Ssverity. Level IV violation for failure to adhere to or '
improvements implemented during the assessment period.
                                      establish' procedures for performing breathing: zcne air
The licensee developed a detailed program for completed
                                      samples and for exposure control during steam generator
l
                                      work.  (08-31-02)
L
                              b.    Severity Level IV violation for failure to evaluate
maintenance record review, which is quite thorough and effective
                                      the radiation hazards present in the 690 foot eleva-
                                      tion Pipe Chase in the Auxiliary Buildine.                                                      (89-05-04)
                              2..    Performance Rating:
                                      Category 2
                              3.    Recommendations:
      .
                                    ' Hone                                                                                                          .
                  C.  Maintenance / Surveillance
                    .1.      Analysis
                              During the assessment period, the technical quality of main-
                              tenance and surveillance at Sequoyah was good as a result of the
                              many technical and programmatic upgrades which occurred. These                                                          l
                              programs experienced substantial organizational and~ perscnnel
                              changes resulting in a large number of licensee initiatives.
                              The addition of a new maintenance superintendent at the
                              beginning of the assessment period . resulted in licensee
                              initiatives in the maintenance area which included; increasing
                              the use of system engineers, the use of.new vibration monitoring
                              equipment techniques, maintenance procedure enhancement,
                              extensive Motor Operated Valve Actuators (M0 VATS) testing of
                              primary and balance-of-plant valves, establishment of a 24 hour
                              Outage Manager to coordinate maintenance and triodification work,
                              and the organization of maintenance and modification activities                                                        l
                              into train and system outages.                                Management of the Maintenance
                              Program was very effective as demonstrated by positive trends in
                              industry indicatcrs such as maintenance backlog, tagging,
                              overtime use, CAQR and LER generation, QA document rejection,
                              Post Modification Testing (PMT) rejection requiring maintenance
                                                      _ _ _ _ _ _ _ _ - _ _ _ - _ _ _          - _ _ _ _ _ _ _ _ _ _ _ _ _ _ -
 
        - - . __                                                                                                            _-                  -_                                                                                                _
                                                                                                                                                                                                                                                        . .
                -
    .
      .
  ~
                                                                                                                                                          31
                                                                                                                              rework, personnel contamination, industrial safety practices,
                                                                                                                              and delinquent safety-related preventive maintenance. Line
                                                                                                                              management increased its presence in the operating and work
                                                                                                                              spaces, became more aware of plant status and technical issues
                                                                                                                              and demonstrated a. commitment to the program and associated
                                                                                                                              improvements implemented during the assessment period.
l
l
                                                                                                                              The licensee developed a detailed program for completed
in identifying and correcting deficiencies.
L                                                                                                                              maintenance record review, which is quite thorough and effective
The use of
l                                                                                                                              in identifying and correcting deficiencies.                                 The use of
procedures in accomplishing maintenance activities was adequate
                                                                                                                              procedures in accomplishing maintenance activities was adequate
and improving. The quality of procedures and work requests, and
                                                                                                                              and improving. The quality of procedures and work requests, and
their associated review, steadily increased as a result of
                                                                                                                              their associated review, steadily increased as a result of
Maintenance Section upper and middle level management
                                                                                                                              Maintenance Section upper and middle level management
involvement in the licensee's program for removal, repair and
                                                                                                                              involvement in the licensee's program for removal, repair and
restoration of safety-related equipment. The licensee initiated
                                                                                                                              restoration of safety-related equipment. The licensee initiated
a system / train outage concept which was coordinated with unique
                                                                                                                              a system / train outage concept which was coordinated with unique
site electrical distribution and TS requirements.
                                                                                                                              site electrical distribution and TS requirements.                                                           In addition,
In addition,
                                                                                                                              the licensee instituted a standard maintenance practice which
the licensee instituted a standard maintenance practice which
                                                                                                                              established the niethod for managing, tracking, planning,
established the niethod for managing, tracking, planning,
                                                                                                                              scheduling, post work evaluation of and documentation of main-
scheduling, post work evaluation of and documentation of main-
                                                                                                                              tenance work activities. This establishment of administrative
tenance work activities.
                                                                                                                              control over maintenance work activities reduced open-ended
This establishment of administrative
                                                                                                                              " Troubleshoot and Repair" type work orders and provided clearer
control over maintenance work activities reduced open-ended
                                                                                                                              direction to the personnel performing work in the field.
" Troubleshoot and Repair" type work orders and provided clearer
                                                                                                                              Operability determination was also added to the administrative
direction to the personnel performing work in the field.
                                                                                                                              control process prior to closing out work orders.
Operability determination was also added to the administrative
                                                                                                                              The licensee's action with regard to NRC maintenance related
control process prior to closing out work orders.
                                                                                                                              initiatives was generally good. The response varied depending
The licensee's action with regard to NRC maintenance related
                                                                                                                              on the organizations involved and the time during the assess-
initiatives was generally good.
                                                                                                                              ment peciod when the NRC initiatives occurred.                                                                 Licensee
The response varied depending
                                                                                                                              response improved in all areas throughout the assessment
on the organizations involved and the time during the assess-
                                                                                                                              period. Responses from onsite maintenance and modifications
ment peciod when the NRC initiatives occurred.
                                                                                                                              organizations were usually quick, professional and technically
Licensee
                                                                                                                              accurate. During the initial portion of the SALP assessment
response improved in all areas throughout the assessment
                                                                                                                              period, support for onsite maintenance related issues from the
period.
                                                                                                                              TVA DNE organization took long periods of time. This caused
Responses from onsite maintenance and modifications
                                                                                                                              issue resolution and operability determination to lag.
organizations were usually quick, professional and technically
                                                                                                                              However, by the middle of the assessment period DNE support
accurate.
                                                                                                                              for maintenance and modification activities was much improved.
During the initial portion of the SALP assessment
                                                                                                                              Licensee resolution of maintenance related technical issues
period, support for onsite maintenance related issues from the
                                                                                                                              usually indicated technical understanding of the issues,
TVA DNE organization took long periods of time.
                                                                                                                              operational conservatism, and was generally well thought out.
This caused
                                                                                                                              Examples of well thought out maintenance activities were;
issue resolution and operability determination to lag.
                                                                                                                              RCP trip bus troubleshooting and repair, and steam generator
However, by the middle of the assessment period DNE support
                                                                                                                              tube leak resolution and preventive plugging.                                             Those main-
for maintenance and modification activities was much improved.
                                                                                                                                tenance activities that were less professionally addressed
Licensee resolution of maintenance related technical issues
                                                                                                                              by the licensee included pressurizer safety valve trip
usually indicated technical understanding of the issues,
                                                                                                                              setpoint calibrations which occurred at the beginning of
operational conservatism, and was generally well thought out.
                                                                                                                              the assessment period.
Examples of well thought out maintenance activities were;
                  _ _ - - _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ - - - _ - _ - _ _ - _ _ _ _ _ - _ _ - _ _ _                                               .___ - _ _ _ _ _ _ _ _ - _ _ _ - _ _ _ _ - - _ _ _ - - - - - - _ _ -
RCP trip bus troubleshooting and repair, and steam generator
tube leak resolution and preventive plugging.
Those main-
tenance activities that were less professionally addressed
by the licensee included pressurizer safety valve trip
setpoint calibrations which occurred at the beginning of
the assessment period.
_ _ - - _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ - - - _ - _ - _ _ - _ _ _ _ _ - _ _ - _ _ _
.___
- _ _ _ _ _ _ _ _ - _ _ _ - _ _ _ _ - - _ _ _ - - - - - - _ _ -


                                                                                                                                                                                          __ ._ -
__ ._ -
m <
-j
                                                                                .                                                                                                               -j
<
      '
m
  .                                                                                                                                                                                               t
.
    '
'
h'                                                                           32
t
          The maintenance staff is generally well qualified and trained.
.
          Special training was given to maintenance personnel following                                                                                                                             4
'
          issues related to the maintenance management system, EQ, conduct                                                                                                                         {
h'
          of testing, and configuration control. Trrining also included                                                                                                                           j
32
          management training for all levels of liaintenance Department                                                                                                                             i
The maintenance staff is generally well qualified and trained.
          management and specific technical training for first and second
Special training was given to maintenance personnel following
          line managers to increase in-craft and cross-craft supervisory
4
          expertise. The experience levels of maintenance department
issues related to the maintenance management system, EQ, conduct
          first line supervisors averaged approximately 10 years of craft
{
          related experience, which included several hundred hours of
of testing, and configuration control.
          craft and engineering training. The site maintained the INPO
Trrining also included
          training accreditation reccived during the basii period for
j
          maintenance training.
management training for all levels of liaintenance Department
          During the assessment period, outage and work control
i
          processes were established and implemented.                                                                                                         Performance
management and specific technical training for first and second
          immediately improved due to planning and assignment of
line managers to increase in-craft and cross-craft supervisory
          priorities. Procedures for control of these processes were well
expertise.
          defined, and appeared to be understood by the personnel involved
The experience levels of maintenance department
          in their implementation. The technical background and level of
first line supervisors averaged approximately 10 years of craft
          plant systems knowledge of the planners, coordinators and
related experience, which included several hundred hours of
          managers in the work control / outage organization was excellent.
craft and engineering training.
          These positions were filled with operators, engineers, and
The site maintained the INPO
          managers that were deeply involved in the day-to-day operations
training accreditation reccived during the basii period for
          of the plant and demonstrated excellent communications and
maintenance training.
          organizational skills.
During the assessment period, outage and work control
        '
processes were established and implemented.
'          While maintenance tracking and planning was considered a
Performance
          strength, maintenance outage stheduling was considered to be a
immediately improved due to planning and assignment of
          weakness. The licensee demonstrated it was capable of drafting
priorities.
          detailed correct 1<e and diagnostic niaintenance plans, and                                                                                                                             1
Procedures for control of these processes were well
          implementing those plans in the field. However, outage and
defined, and appeared to be understood by the personnel involved
          maintenance schedules rarely had any realistic relation to the
in their implementation.
          actual work being performed in the plant and exhibited continual
The technical background and level of
          and predictable schedule slips.
plant systems knowledge of the planners, coordinators and
          The licensee used the composite maintenance crew concept for
managers in the work control / outage organization was excellent.
          NOVATS testing, refrigeration, and general maintenance. An NRC
These positions were filled with operators, engineers, and
            review of the implementation of the composite crew process at
managers that were deeply involved in the day-to-day operations
          the begining of the assessement period revealed that no
of the plant and demonstrated excellent communications and
          procedures addressed the training and qualifications require-                                                                                                                           j
organizational skills.
          ments for foremen supervising personnel in other crafts, for
'
                                                                                                                                                                                                  '
While maintenance tracking and planning was considered a
          craftsmen performing work outside of their craft, or for
'
          craftsmen performing independent verification outside of their
strength, maintenance outage stheduling was considered to be a
          craft.   Although no plant events were attributable to composite
weakness.
          crews during the assessment period, composite maintenance crews
The licensee demonstrated it was capable of drafting
          existed in, contradiction to the training and qualification
detailed correct 1<e and diagnostic niaintenance plans, and
            requirements for maintenance foremen and craftsmen. This
1
            indicated insufficient management attention to and involvement
implementing those plans in the field.
          with the composite crew concept and represented a failure by
However, outage and
          management to recognize that minimum regulatory requirements
maintenance schedules rarely had any realistic relation to the
                                                                                                                                                                                                  ;
actual work being performed in the plant and exhibited continual
                        _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ . _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ . _ . _ _ _ _ _ _ _ _ _ _ _ _ _ _
and predictable schedule slips.
The licensee used the composite maintenance crew concept for
NOVATS testing, refrigeration, and general maintenance. An NRC
review of the implementation of the composite crew process at
the begining of the assessement period revealed that no
procedures addressed the training and qualifications require-
j
ments for foremen supervising personnel in other crafts, for
'
craftsmen performing work outside of their craft, or for
craftsmen performing independent verification outside of their
craft.
Although no plant events were attributable to composite
crews during the assessment period, composite maintenance crews
existed in, contradiction to the training and qualification
requirements for maintenance foremen and craftsmen. This
indicated insufficient management attention to and involvement
with the composite crew concept and represented a failure by
management to recognize that minimum regulatory requirements
;
_ _ _ _ _ _
_ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _
_ . _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ . _ . _ _ _ _ _ _ _ _ _ _ _ _ _ _


            _
,
              _ _ - - -           -   .               . _ _ _   _. .. - ._       __       . _ _ _ _
_
      ,
_ _ - - -
        -
-
          4
.
        .
. _ _ _
    '
_. ..
                                                  33
-
                          were not being met. Once management attention was focused on-the
._
                                ~
__
                          problem, a comprehensive procedure was developed to address the
. _ _ _ _
                          composite maintenance crew concept. Corrective actions that
-
                          were initiated appeared to have resolved problems with the
4
                          composite crew concept.
.
                          The. control and use of calibrated equipment met regulatory
                          requirements and purchase receipt inspection and traceability of
                          installed materials was found to be acceptable. Additionally,
                        Lpost maintenance testing was found to be satisfactorily
                          accomplished.
                          During the assessment period the material condition of
                        . plant components steadily improved. A review of system failures
                          did not indicate any adverse management or maintenance
                          practices. Several conditions that did not constitute failures
                          but did affect plant operations were: leaking pressurizer safety
                          valves on both units, a leaking reactor vessel flange 0-ring on-
                          Unit 1, and unstable feedwater automatic controls for both
                          units. In the case of the Unit 1 pressurizer safeties and the
                          Unit 1 vessel flange ~ 0-ring, plant activities were well
                          controlled and personnel involved were technically astute and
                          receptive to NRC initiatives.          However, in reference to
                          feedwater controls, less than cohesive disciplined management
                          activities were'noted.
.                        The plant's material condition, preservation, and housekeeping
                          status was adequate. Occasionally maintenance debris and other
                          material / housekeeping deficiencies existed in the auxiliary
                        L bu11 ding and other plant spaces. Additionally, work in progress
                          was often left open, uncovered, and unattended during work crew
                          breaks and turnover periods, Examples of these ccnditions were;
                          ice condenser cleanliness prior to Unit 2 initial heatup, loose
                          items and debris found by the NRC in safety-related electrical
                          panels and distribution boards.
'
'
                          During the assessment period the Preventive Maintenance
33
                          (PM) program at Sequoyah was in the midst of a significant
were not being met. Once management attention was focused on-the
                          amount of change.   The licensee initiated a PM Upgrade Program
~
                          which was very detailed and resulted in a significant increase
problem, a comprehensive procedure was developed to address the
                          in' the number of PMs required for plant equipment. This PM
composite maintenance crew concept.
                          upgrade effort was in place for the majority of the assess-
Corrective actions that
                          ment period and the developmental stage will last another year.
were initiated appeared to have resolved problems with the
                          Weaknesses were identified in the number of outstanding
composite crew concept.
                          delinquent PMs, and the existence of a significant percentage of
The. control and use of calibrated equipment met regulatory
                          recently developed PMs that had never actually been performed on
requirements and purchase receipt inspection and traceability of
                          plant equipment. The everall conclusion in the Pti area was that     -
installed materials was found to be acceptable.
                          a very strong PM program was being developed with involved
Additionally,
                          management support. The program is being developed as a quality
Lpost maintenance testing was found to be satisfactorily
                          activity and will improve the safety and reliability of plant
accomplished.
                          equipment when it is fully impleme 'ed. The results of this
During the assessment period the material condition of
                          effort, in the form of benefit to       tant equipment, has r.ot yet
. plant components steadily improved. A review of system failures
                          been realized.                                                                 .
did not indicate any adverse management or maintenance
  i
practices.
Several conditions that did not constitute failures
but did affect plant operations were: leaking pressurizer safety
valves on both units, a leaking reactor vessel flange 0-ring on-
Unit 1, and unstable feedwater automatic controls for both
units.
In the case of the Unit 1 pressurizer safeties and the
Unit 1 vessel flange ~ 0-ring, plant activities were well
controlled and personnel involved were technically astute and
receptive to NRC initiatives.
However, in reference to
feedwater controls, less than cohesive disciplined management
activities were'noted.
The plant's material condition, preservation, and housekeeping
.
status was adequate. Occasionally maintenance debris and other
material / housekeeping deficiencies existed in the auxiliary
L bu11 ding and other plant spaces.
Additionally, work in progress
was often left open, uncovered, and unattended during work crew
breaks and turnover periods, Examples of these ccnditions were;
ice condenser cleanliness prior to Unit 2 initial heatup, loose
items and debris found by the NRC in safety-related electrical
panels and distribution boards.
During the assessment period the Preventive Maintenance
'
(PM) program at Sequoyah was in the midst of a significant
amount of change.
The licensee initiated a PM Upgrade Program
which was very detailed and resulted in a significant increase
in' the number of PMs required for plant equipment.
This PM
upgrade effort was in place for the majority of the assess-
ment period and the developmental stage will last another year.
Weaknesses were identified in the number of outstanding
delinquent PMs, and the existence of a significant percentage of
recently developed PMs that had never actually been performed on
plant equipment.
The everall conclusion in the Pti area was that
-
a very strong PM program was being developed with involved
management support. The program is being developed as a quality
activity and will improve the safety and reliability of plant
equipment when it is fully impleme 'ed.
The results of this
effort, in the form of benefit to
tant equipment, has r.ot yet
been realized.
.
i


-_ - -_                                                             __
-_ - -_
                                                                                                            .
__
                                                                                                                                              -
.
        ..
I
          -
-
                                                                                                                                                                                            I
-
        -
..
L V                                                                                                                                             34'
-
  ,
L V
                                                                                                                      Predictive- analysis techniques were well integrated into the
34'
                                                                                                                      licensee's maintenance program.       Vibration analysis and M0 VATS
,
                                                                                                                      testing .were active at the site and were found to be
Predictive- analysis techniques were well integrated into the
                                                                                                                      instrumental- in the. identification of much of the corrective
licensee's maintenance program.
                                                                                                                    maintenance.     These two techniques were also found to be used as
Vibration analysis and M0 VATS
                                                                                                                      an integral part of the licensee's post-maintenance surveillance
testing .were active at the site and were found to be
                                                                                                                      activities.     In addition, the licensee implemented a- system
instrumental- in the. identification of much of the corrective
                                                                                                                    performance monitoring program to improve station reliability.
maintenance.
                                                                                                                    The program includes vibration monitoring, system and component
These two techniques were also found to be used as
                                                                                                                  . parameter trending, System of the Month reviews, and performance
an integral part of the licensee's post-maintenance surveillance
                                                                                                                    walkdowns.     Upper plant management is very attuned to the
activities.
                                                                                                                      results from these maintenance techniques and plant operational
In addition, the licensee implemented a- system
                                                                                                                      decisions were made using this data.
performance monitoring program to improve station reliability.
                                                                                                                    At the beginning of the assessment period, ' management
The program includes vibration monitoring, system and component
                                                                                                                      continued to experience' a lack of . full understanding of the
. parameter trending, System of the Month reviews, and performance
                                                                                                                      technical requirements necessary to fully resolve some NRC
walkdowns.
                                                                                                                      identified procurement issues. Following NRC identified adjust-
Upper plant management is very attuned to the
                                                                                                                    ments to the program, Sequoyah established an acceptable program
results from these maintenance techniques and plant operational
                                                                                                                      for resolving replacement part issues. Following the NRC
decisions were made using this data.
                                                                                                                      findings, management demonstrated a clear understanding of the
At the beginning of the assessment period, ' management
                                                                                                                      issues involved, proposed timely resolution of the findings, and
continued to experience' a lack of . full understanding of the
                                                                                                                      proposed resolutions which were . technically sound.- In a
technical requirements necessary to fully resolve some NRC
                                                                                                                      specific case (e.g., molded case circuit breakers), Sequoyah          I
identified procurement issues.
                                                                                                                      exceeded the. bulletin response requirements which enabled the
Following NRC identified adjust-
                                                                                                                      NRC to provide up-to-date. guidance ' to other licensees. In
ments to the program, Sequoyah established an acceptable program
                                                                                                                      addition, procurement and maintenance management coordinated
for resolving replacement part issues.
                                                                                                                      closely during the second half of the assessment period to          ,
Following the NRC
                                                                                                                      reduce, by approximately 50 percent, the outage work that could
findings, management demonstrated a clear understanding of the
                                                                                                                      not be performed due to outstanding material items.
issues involved, proposed timely resolution of the findings, and
                                                                                                                      Safety-related equipment storage continued to be well managed        ,
proposed resolutions which were . technically sound.-
                                                                                                                      throughout the assessment period.        Several cases existed
In a
                                                                                                                      where detailed storage and material information was necessary to
                                                                                                                      support plant operability determinations. In each case the
                                                                                                                        information was retrieved, clearly' supported operability and
                                                                                                                      demonstrated a service related role for the storage and
                                                                                                                      procurement organizations.
                                                                                                                      Staffing in the procurement and storage areas was adequate.
                                                                                                                      Staffing of the contract engineering group (CEG) was generally
                                                                                                                      good. While site and corporate management had the expertise for
                                                                                                                        the procurement operation, potential impacts on continued
                                                                                                                        performance were identified as a result of their possible
                                                                                                                        involvement in other TVA' site procurement activities.
I
I
                                                                                                                      During this assessment period, Sequoyah transitioned from a
specific case (e.g., molded case circuit breakers), Sequoyah
                                                                                                                        separate dedicated EQ organization to a matrix organization
exceeded the. bulletin response requirements which enabled the
                                                                                                                      within the site DNE organization. This transition occured without
NRC to provide up-to-date. guidance ' to other licensees.
                                                                                                                        interruption or degradation of the quality of EQ corrective and
In
addition, procurement and maintenance management coordinated
closely during the second half of the assessment period to
,
reduce, by approximately 50 percent, the outage work that could
not be performed due to outstanding material items.
Safety-related equipment storage continued to be well managed
,
throughout the assessment period.
Several cases existed
where detailed storage and material information was necessary to
support plant operability determinations.
In each case the
information was retrieved, clearly' supported operability and
demonstrated a service related role for the storage and
procurement organizations.
Staffing in the procurement and storage areas was adequate.
Staffing of the contract engineering group (CEG) was generally
good. While site and corporate management had the expertise for
the procurement operation, potential impacts on continued
performance were identified as a result of their possible
involvement in other TVA' site procurement activities.
I
During this assessment period, Sequoyah transitioned from a
separate dedicated EQ organization to a matrix organization
within the site DNE organization. This transition occured without
interruption or degradation of the quality of EQ corrective and
l
l
l:                                                                                                                         -
l:
            _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ - _ - _ _ _ - _ _ _ - _ _ _ _ _ - _ _ - _ _ _ _ _ _ _ _ _ - _ _
-
_ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ - _ - _ _ _ - _ _ _ - _ _ _ _ _ - _ _ - _ _ _ _ _ _ _ _ _ - _ _


                              ._
._
  _
_
;     .
;
                              .
.
.
1
1
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1
1
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l                                                        35
35
                                  preventive maintenance implementation.   EQ maintenance decisions
*
                                  were made at appropriate levels.       Additionally, plant
preventive maintenance implementation.
                                  organizations had well stated policies to guide them in
EQ maintenance decisions
                                  completing   field work.     Management authority   and
were made at appropriate levels.
                                  responsibilities were defined and understood in the EQ area.
Additionally, plant
                                  Sequoyah management continued their resolution of technical
organizations had well stated policies to guide them in
                                  issues in the maintenance area with conservative approaches
completing
                                  during the assessment period. This was illustrated by the
field
                                  implementation of corrective maintenance activities to support
work.
                                  the qualification of silicone rubber electric cable installed
Management
                                  inside containment and the qualification of transmitter cable
authority
                                  nylon butt splices. The maintenance department was adequately
and
                                  staffed with personnel having the appropriate expertise.
responsibilities were defined and understood in the EQ area.
                                  Surveillance performance and technical adequacy continued to
Sequoyah management continued their resolution of technical
                                  improve through an extensive surveillance review and inplant
issues in the maintenance area with conservative approaches
                                  validation process that continued throughout the assessment
during the assessment period.
                                  period. Surveillance scheduling was reorganized resulting in
This was illustrated by the
                                  only one administrative 1y late TS required surveillance
implementation of corrective maintenance activities to support
                                  occurring following the restart of Unit 1. This improvement in
the qualification of silicone rubber electric cable installed
                                  surveillance management was the result of the licensee's
inside containment and the qualification of transmitter cable
                                  aggressive SI planning and scheduling program. The licensee's
nylon butt splices.
                                  scheduling performance of non-TS required surveillance and
The maintenance department was adequately
                                  preventive maintenance is less aggressive and appears to rely
staffed with personnel having the appropriate expertise.
                                  heavily on input from upper plant management rather than first
Surveillance performance and technical adequacy continued to
                                  and second line supervision.
improve through an extensive surveillance review and inplant
                                  In the vast majority of surveillcoces performed implementation
validation process that continued throughout the assessment
                                  of the surveillance testing was excellent reflecting adequate
period.
                                  planning and assignment of priorities, and indicating an
Surveillance scheduling was reorganized resulting in
                                  aggressive level of management overview. However, surveillance
only one administrative 1y late TS required surveillance
                                  procedural adherence problems continued throughout the assess-
occurring following the restart of Unit 1.
                                  ment period, although improvement in this area was noted         I
This improvement in
                                  following the initial Unit 2 restart activities.     Exampl'es of
surveillance management was the result of the licensee's
                                  procedural adherence problems were; surveillance of a Reactor
aggressive SI planning and scheduling program.
                                  Coolant System (RCS) flow indicator resulting in a reactor trip
The licensee's
                                  when the instrument was returned to service, and a power operated
scheduling performance of non-TS required surveillance
                                  relief valve (PORV) opening when an RCS resistance teniperature
and
                                  device (RTD) was returned to service. Licensee resolution of
preventive maintenance is less aggressive and appears to rely
                                  surveillance related technical issues reflected a thorough
heavily on input from upper plant management rather than first
                                  understanding of the appropriate issues. Management was
and second line supervision.
                                  responsive to NRC initiatives in that they established new
In the vast majority of surveillcoces performed implementation
                                  surveillance instructions in response to NRC information notices I
of the surveillance testing was excellent reflecting adequate
                                  and bulletins. Personnel performing as test directors while
planning and assignment of priorities, and indicating an
                                  conducting surveillance testing activities appeared to have a
aggressive level of management overview.
                                  good working knowledge of the surveilltrce procedures and were
However, surveillance
                                  trained in the use of required instrumentation.
procedural adherence problems continued throughout the assess-
        _ _ _ - _ - - _ - _ _
ment period, although improvement in this area was noted
I
following the initial Unit 2 restart activities.
Exampl'es of
procedural adherence problems were; surveillance of a Reactor
Coolant System (RCS) flow indicator resulting in a reactor trip
when the instrument was returned to service, and a power operated
relief valve (PORV) opening when an RCS resistance teniperature
device (RTD) was returned to service.
Licensee resolution of
surveillance related technical issues reflected a thorough
understanding of the appropriate issues.
Management was
responsive to NRC initiatives in that they established new
surveillance instructions in response to NRC information notices
I
and bulletins.
Personnel performing as test directors while
conducting surveillance testing activities appeared to have a
good working knowledge of the surveilltrce procedures and were
trained in the use of required instrumentation.
_ _ _ - _ - - _ - _ _


__
__
      :%
:%
    .
.
  '
36
                                  36
'
          A management initiative, designed to minimize the recurrence of
A management initiative, designed to minimize the recurrence of
          mispositioned valves, was to form a dedicated Operations
mispositioned valves, was to form a dedicated Operations
          Department surveillance instruction performance team. Forming
Department surveillance instruction performance team.
          such a team limited the number of people performing surveillance
Forming
          instructions, increased the exposure of each team member to the
such a team limited the number of people performing surveillance
          various instructions, and enhanced internal communications. The
instructions, increased the exposure of each team member to the
          team appeared to be effective in improving efficiency and
various instructions, and enhanced internal communications.
          control. The SI team concept was a case of effective technical
The
          resolution and management involvement that occurred during the
team appeared to be effective in improving efficiency and
          assessment period.                       ,
control.
          During the assessment period physics-related activities
The SI team concept was a case of effective technical
          associated with the restart of Units 1 and 2 demonstrated the
resolution and management involvement that occurred during the
          ability of the licensee to perform at a technical level above
assessment period.
          that required to meet regulatory requirements. A number of
,
          complications were experienced during startup testing, including
During the assessment period physics-related activities
          significant differences between the measured and predicted
associated with the restart of Units 1 and 2 demonstrated the
          critical boron concentrations on both units and a positive zero
ability of the licensee to perform at a technical level above
          power moderator coefficient on Unit 1. Licensee management
that required to meet regulatory requirements.
          responded effectively to the complications which were
A number of
          encountered.       Management ensured that' adequate personnel
complications were experienced during startup testing, including
          resources were allocated to properly perform the test program
significant differences between the measured and predicted
          and that an atmosphere existed which encouraged feedback from
critical boron concentrations on both units and a positive zero
          the ~ersonnel invohed with the testing.             This resulted in a
power moderator coefficient on Unit 1.
          continuing improvement of the reactor physics testing program.
Licensee management
-
responded effectively to the complications which were
          A significant investment was made in the training of 'inexperi-
encountered.
          enced personnel and in the cross training of design specialists,
Management ensured that' adequate personnel
          which should benefit future reactor engineering activities
resources were allocated to properly perform the test program
          and result in further improvement of the program. Marked
and that an atmosphere existed which encouraged feedback from
          improvement in the control of nuclear design calculations
the ~ersonnel invohed with the testing.
          and computer codes was observed during the assessment period.
This resulted in a
          Management involvement in assuring quality was demonstrated in
continuing improvement of the reactor physics testing program.
          that the chemistry program was very actively supported by the
A significant investment was made in the training of 'inexperi-
          corporate chemistry staff. The staff was involved in developing
-
          a corporate policy statement and directive which established
enced personnel and in the cross training of design specialists,
          philosophy, directives and responsibilities for a chemistry
which should benefit future reactor engineering activities
          program which endorsed the guidelines recommended by the steam
and result in further improvement of the program.
          generators owners group (SG0G) and Electric Power Research
Marked
          Institute (EPRI). Management emphasized the need for quality
improvement in the control of nuclear design calculations
          control in all aspects of the chemistry program to meet the
and computer codes was observed during the assessment period.
          stringent criteria recommended by SG0G and EPRI for prevention
Management involvement in assuring quality was demonstrated in
          of corrosion.
that the chemistry program was very actively supported by the
          Adequate resolution of technical issues was exhibited in the                                                           ,,
corporate chemistry staff. The staff was involved in developing
          short term wet layup of Unit 2, the long term dry layup of
a corporate policy statement and directive which established
          Unit 3 and the startup of Unit 2. Modifications to the moisture
philosophy, directives and responsibilities for a chemistry
          separator reheaters replaced copper-nickel tubes with stainless
program which endorsed the guidelines recommended by the steam
          steel tubes, reducing the potential sour.ce of copper corrosion
generators owners group (SG0G) and Electric Power Research
          prcducts to the steam generators. Replacement of all resins in
Institute (EPRI).
          the polisher vessels prior to restart of Unit 2 was a
Management emphasized the need for quality
                                                                                                                                    -
control in all aspects of the chemistry program to meet the
                                                      _ - _ - _ - _ - - _ _ _ _ _ . _ _ _ . _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _
stringent criteria recommended by SG0G and EPRI for prevention
of corrosion.
Adequate resolution of technical issues was exhibited in the
,,
short term wet layup of Unit 2, the long term dry layup of
Unit 3 and the startup of Unit 2.
Modifications to the moisture
separator reheaters replaced copper-nickel tubes with stainless
steel tubes, reducing the potential sour.ce of copper corrosion
prcducts to the steam generators.
Replacement of all resins in
the polisher vessels prior to restart of Unit 2 was a
-
_ - _ - _ - _ - - _ _ _ _ _ . _ _ _ . _ _
_ _ _ _ _ _ _ _ _ _ _ _ _ _ _
_


                                                                                                                                                                                                            __ -____-__
__ -____-__
            ~
~
    .
.
      .
  -
                                                                    37
                                                                                                                                                                    '
.
.
                                contributing factor to the good water quality during restart.
37
                                Consequently, a lengthy chemistry hold was not necessary.                                                                                                                             .
-
                                However, the shortage of demineralized water limits the nunber
.
                                of polishers that can be used.                                                                       The ' licensee has initiated
'
                                investigatory programs to improve the all volatile treatment
contributing factor to the good water quality during restart.
                                -(AVT) chemistry control program.                                                                     The areas of wet and dry layup
Consequently, a lengthy chemistry hold was not necessary.
                                of plant systems, and corrosion and erosion progrems were
.
                                determined to be acceptable.
However, the shortage of demineralized water limits the nunber
                                Even though there were major changes in key staffing positions
of polishers that can be used.
                                in the plant water chemistry program, the defined program was
The ' licensee has initiated
                                implemented with an adequate number of qualified, experienced
investigatory programs to improve the all volatile treatment
                                supervisors in accordance with licensee procedures.
-(AVT) chemistry control program.
                                As determined at the end of the assessment period, the ISI
The areas of wet and dry layup
                                program and procedures were acceptable and management
of plant systems, and corrosion and erosion progrems were
                                involvement in the ISI process was apparent. Based on a review
determined to be acceptable.
                                of ISI program submittals and program changes, TVA's responsive-
Even though there were major changes in key staffing positions
                                ness to NRC initiatives and staffing for ISI work was adequate.
in the plant water chemistry program, the defined program was
                                During the assessment period the Inserv'ce Test (IST)
implemented with an adequate number of qualified, experienced
                                program and records were greatly improved and preclude the
supervisors in accordance with licensee procedures.
                                problems identified during the basis period. Management
As determined at the end of the assessment period, the ISI
                                appeared to be involved in assuring quality in IST activities.
program and procedures were acceptable and management
                                Responsiveness to NRC initiatives was evident. Based on
involvement in the ISI process was apparent.
                                observation of in-process testing and review of IST activities,
Based on a review
                                staffing levels appeared to be adequate.                                                                     IST personnel observed
of ISI program submittals and program changes, TVA's responsive-
                                and interviewed in the field conducted themselves in a
ness to NRC initiatives and staffing for ISI work was adequate.
                                professional manner, and appeared to bc well traircd and
During the assessment period the Inserv'ce Test (IST)
                                qualified for their responsibilities.
program and records were greatly improved and preclude the
                                Seventeen violations were identified:
problems identified during the basis period.
                                a.     Severity Level IV violation for failure to have a procedure
Management
                                        for composite maintenance crews.                                                                 (87-78-02)
appeared to be involved in assuring quality in IST activities.
                                b.     Severity Level IV violation for failure to adequately                                                                                                                                             l
Responsiveness to NRC initiatives was evident.
                                        implement surveillance involving RCS temperature,                                                                                                                                                 ;
Based on
                                        containment spray system flow, and ice condenser
observation of in-process testing and review of IST activities,
                                        operability. (88-02-01)
staffing levels appeared to be adequate.
                                c.     Severity Level IV violation for failure to adequately
IST personnel observed
                                        implement work instructions involving resistance
and interviewed in the field conducted themselves in a
                                        temperature detectors, a system hold onder, and the
professional manner, and appeared to bc well traircd and
                                        safety-related air system.                                                                 (88-17-01)
qualified for their responsibilities.
                                d.     Severity Level IV violation for failure to have an adequate
Seventeen violations were identified:
                                        fire protection surveillance instruction for containment
a.
                                        penetration sleeves.                                                 (88-19-01)
Severity Level IV violation for failure to have a procedure
                                e.     Severity Level IV violation for failure to have an adequate                                                                                                                                       ,
for composite maintenance crews.
                                        SI for fire barriers.                                                           (88-19-03)                                                                                                       )
(87-78-02)
                                f.     Severity Level IV violation for failure to establish and
b.
                                        implement plant instructions (TS interpretations) that
Severity Level IV violation for failure to adequately
                                        complied with TS 3.7.1.2.                                                                 (88-20-01)
l
E_-----_-----_--.-_---------_----------------__----____--__ _ - - - _ - - _ _ _ - . - - _ - - - - - - - - - - - - - - - - - - - - -                     - - _ . - - - - - _ - - - - - - - - - - - - - - - -               --_-------. _ - _
implement surveillance
involving RCS temperature,
;
containment spray system flow, and ice condenser
operability.
(88-02-01)
c.
Severity Level IV violation for failure to adequately
implement work instructions involving resistance
temperature detectors, a system hold onder, and the
safety-related air system.
(88-17-01)
d.
Severity Level IV violation for failure to have an adequate
fire protection surveillance instruction for containment
penetration sleeves.
(88-19-01)
e.
Severity Level IV violation for failure to have an adequate
,
SI for fire barriers.
(88-19-03)
)
f.
Severity Level IV violation for failure to establish and
implement plant instructions (TS interpretations) that
complied with TS 3.7.1.2.
(88-20-01)
E_-----_-----_--.-_---------_----------------__----____--__
_ - - - _ - - _ _ _ - . - - _ - - - - - - - - - - - - - - - - - - - - -
- - _ . - - - - - _ - - - - - - - - - - - - - - - -
--_-------. _ - _


      ..         -_         ---       _       - . _ - _ _     _-       _
..
                                                                                  .-.   . - . _   , . _ - _ - _ - _
-_
              I-     *
---
        ...                                                                                     ,
_
                                                                                                                        ]
- . _ - _ _
          ..
_-
  . l- ( i
_
    -
.-.
                                                              38                                                       i
. - . _
                                                                                                                    a
, . _ - _ - _ - _
            ,
I-
                            g.   l Severity. Level IV ' violation for failure to implement                         ~{
]
                                    surveillance requirement 4.5.1.1.1.6 involving cold leg'                           j
*
                                    accumulator boron concentration.         (88-20-02).                               1
...
                            h.   ' Severity Level IV violation for failure to control
,
                                    maintenance activities related to a steam gen:.-ator level
..
                                                                              ~
. l- ( i
                                  . indicator, and flow transmitter 2-FT-68-718 (88-28-01).
-
                            i.     Severity Level IV violation for structural walkdown issues.
38
                                  -(88-29-02)
i
                            j.     Severity Level V violation for failure to control work
a
                                    practices involving' the installation of beveled washers,                       y
g.
                                    spring cans and anchor bolt alignment. (88-29-03)                               -l
l Severity. Level IV ' violation for failure to implement
                            k.     . Severity Level IV violation for failure to perform an.
~
                                    adequate ASME section XI test. (88-29-04)
,
                            1.     Severity Level IV violation for UHI system inoperable due
surveillance requirement 4.5.1.1.1.6 involving cold leg'
                                  .to failure to perform surveillance. (88-34-02)
j
                            m.     Severity Level IV violation for EDG surveillance. not
accumulator boron concentration.
                                    performed when one EDG was made inoperable. (88-34-03)
(88-20-02).
                            n.     Severity Level IV violation for two examples of failure to '
1
                                    follow procedures for radiation monitor work. (88-39-01)'
h.
                            o.     -Severity Level IV violation for failure to have an adequate
' Severity Level IV violation for failure to control
                                    work plan. (88-39-03)
maintenance activities related to a steam gen:.-ator level
                            p.     Severity Level IV violation for failure to follow AI-47
~
                                    requirements. (88-40-01)
. indicator, and flow transmitter 2-FT-68-718 (88-28-01).
                                                                                  '
i.
                            q.     - Severity Level IV violation for failere to follow incore
Severity Level IV violation for structural walkdown issues.
                                    flux detector withdrawal procedures. (88-44-02)
-(88-29-02)
,.                      2. Performance Rating:
j.
                            Category 2
Severity Level V violation for failure to control work
                        3. Recommendations:
practices involving' the installation of beveled washers,
                            The Board recognized that improvements in the maintenance area
y
                            were the direct result of initiatives instituted by the new
spring cans and anchor bolt alignment. (88-29-03)
                            maintenance management.             The Board also recognizes that an
-l
                .          aggressive FM program has been developed, but is not fully                               -
k.
                            implemented, ind that benefit to the equipment has not yet been
. Severity Level IV violation for failure to perform an.
                            realized.
adequate ASME section XI test. (88-29-04)
                    .
1.
                                                                                                                      -
Severity Level IV violation for UHI system inoperable due
.to failure to perform surveillance. (88-34-02)
m.
Severity Level IV violation for EDG surveillance. not
performed when one EDG was made inoperable. (88-34-03)
n.
Severity Level IV violation for two examples of failure to '
follow procedures for radiation monitor work. (88-39-01)'
o.
-Severity Level IV violation for failure to have an adequate
work plan. (88-39-03)
p.
Severity Level IV violation for failure to follow AI-47
requirements. (88-40-01)
'
q.
- Severity Level IV violation for failere to follow incore
flux detector withdrawal procedures. (88-44-02)
2.
Performance Rating:
,.
Category 2
3.
Recommendations:
The Board recognized that improvements in the maintenance area
were the direct result of initiatives instituted by the new
maintenance management.
The Board also recognizes that an
aggressive FM program has been developed, but is not fully
implemented, ind that benefit to the equipment has not yet been
-
.
realized.
.
-
I
I
,
,


                                                                        _-__ _ __ _ __ _ -
_-__ _ __ _ __ _ -
r
r
l-   ..-
l-
      *
. . -
                                                                                                    .
*
    <                                     39
.
          D. Emergency Preparedness
<
  ''
39
            1. Analysis
D.
      ,          The inspections conducted curing this assessment period ir.cluded
Emergency Preparedness
        i         two routine Emergency Preparedness (EP) inspections and a full
''
                  participation EP exercise.                                                                 .
1.
                  The routine EP inspection performed March 7-11, 1988, disclosed
Analysis
                  that the licensee had revised its system for reviewing and
The inspections conducted curing this assessment period ir.cluded
                  approving changes to the Radiological Emergency Plan and
,
                  Implementing Procedures. The inspection noted that the changes
i
                  made under the new system were being properly cpproved and
two routine Emergency Preparedness (EP) inspections and a full
                  distributed in a timely manner.       Emergency supplies and
participation EP exercise.
                  equipment met regulatory requirements. Although several key
.
                  personnel changes had occurred, personnel had been properly
The routine EP inspection performed March 7-11, 1988, disclosed
                  trained prior to integration into the emergency response
that the licensee had revised its system for reviewing and
                  organization with one exception.     The exception resulted in a
approving changes to the Radiological Emergency Plan and
                  violation for failure to provide annual retraining to an
Implementing Procedures.
                  alternate Technical Support Center communicator. In the EP
The inspection noted that the changes
                  area, preparedness audits were found to meet regulatory require-
made under the new system were being properly cpproved and
                  ments.
distributed in a timely manner.
                  The routine EP inspection performed Septernber 1-4, 1988,
Emergency supplies and
                  discicsed that the licensee hcd declared six Notification of
equipment met regulatory requirements.
                  Unusual Events (!!OUE) since February 4,1988.     All events were
Although several key
                  promptly classified with the exception of a " seismic alarn
personnel changes had occurred, personnel had been properly
                  received" on February 8, 1988. The licensee's failure to
trained prior to integration into the emergency response
                  promptly report this event as an NOUE was identified as a
organization with one exception.
                  violation for failure to adequately -implement an emergency
The exception resulted in a
                  procedure. In addition, a second example of failure to prcmptly
violation for failure to provide annual retraining to an
                  declare an NOUE en high RCS leak rate wcs also identified. The
alternate Technical Support Center communicator.
                  licensee was maintaining an adequate notifications and commun-
In the EP
                  ications capability in the event of an emergency. The areas of
area, preparedness audits were found to meet regulatory require-
                  shift staffing and augmentation, training, and dose calculation
ments.
<                and assessment were found to be adequate ~.
The routine EP inspection performed Septernber 1-4,
                  The emergency exercise with full participation was conducte.d on
1988,
                  December 14, 1988, and demonstrated that the licensee could
discicsed that the licensee hcd declared six Notification of
                  satisfactorily respond to an emergency at the facility. The
Unusual Events (!!OUE) since February 4,1988.
                  most significant of the negative observations was a failure of
All events were
                  the Shift Operating Supervisor to recognize an explosion as an
promptly classified with the exception of a " seismic alarn
                  entry into the emergency classification logic. However, the
received" on February 8,
                  licensec adequately demonstrated the ability to classify higher
1988.
                  levels of emergency after entering the emergency classification
The licensee's failure to
                  logic. The overall performance was fully satisfactory and an
promptly report this event as an NOUE was identified as a
                  adequate critique was conducted by the licensee,
violation for failure to adequately -implement an emergency
                                                                                                                      i
procedure.
                                                                                __-_-__-_______-_____.____-_______-___a
In addition, a second example of failure to prcmptly
declare an NOUE en high RCS leak rate wcs also identified.
The
licensee was maintaining an adequate notifications and commun-
ications capability in the event of an emergency.
The areas of
shift staffing and augmentation, training, and dose calculation
and assessment were found to be adequate ~.
<
The emergency exercise with full participation was conducte.d on
December 14, 1988, and demonstrated that the licensee could
satisfactorily respond to an emergency at the facility.
The
most significant of the negative observations was a failure of
the Shift Operating Supervisor to recognize an explosion as an
entry into the emergency classification logic.
However, the
licensec adequately demonstrated the ability to classify higher
levels of emergency after entering the emergency classification
logic.
The overall performance was fully satisfactory and an
adequate critique was conducted by the licensee,
i
__-_-__-_______-_____.____-_______-___a


                                                                                                  _ _ _ _ _ _ _ _ _ _ _
_ _ _ _ _ _ _ _ _ _ _
          '
'
  +
+
    .
.
  -
40
                                                          40
-
                                  Three violations were identified.
Three violations were identified.
                                  a.   Severity Level V violation for failure to provide annual
a.
                                        retraining to an alternate Technical Support Center
Severity Level V violation for failure to provide annual
                                      connunicator. (88-18-01)
retraining to an alternate Technical Support Center
                                  b.   Severity Level IV violation for failure to promptly report
connunicator. (88-18-01)
                                      an NOUE when a seismic alarm was received. (88-33-01)
b.
                                  c.   Severity Level IV violation for late reporting of a NOUT on
Severity Level IV violation for failure to promptly report
                                      high RCS leak rate. (88-34-04)
an NOUE when a seismic alarm was received. (88-33-01)
                                  2.   Performance Rating
c.
                                        Categury 2
Severity Level IV violation for late reporting of a NOUT on
                                  3.   Recommendations
high RCS leak rate. (88-34-04)
                                        None
2.
                E. Security
Performance Rating
                  1.             Analysis
Categury 2
                                  During the assessment period three routine security inspec-
3.
            '
Recommendations
  -
None
                                  tions and one special inspection resulted in the issuance of
E.
                                  three licensee-identified-violations relative to key control,
Security
                                  unescorted visitors and officers being found inattentive to
1.
                                  duty. The reactive inspection reviewed the licensee's invest-
Analysis
                                  igation of suspected or alleged drug cbuse and found the
-
                                  licensee's investigation and resolution to be adequate
During the assessment period three routine security inspec-
                                  In February 1988, the licensee performed both an Operational
'
                                  Readiness Review (NSB/CA 88-01) and its annual Quality Assurance
tions and one special inspection resulted in the issuance of
                                  Audit (SSA-88-06) which resulted in the identification of
three licensee-identified-violations relative to key control,
                                  persistent hardware and equipment inadequacies and the continued
unescorted visitors and officers being found inattentive to
                                  dependence on compensatory measures.       While no Conditions
duty.
                                  Adverse to Quality were identified, the Audit concluded that
The reactive inspection reviewed the licensee's invest-
                                  some of the equipment was obsolete and restricted the
igation of suspected or alleged drug cbuse and found the
                                  effectiveness of the security program.     NRC has ascessed the
licensee's investigation and resolution to be adequate
                                  Safeguards Event Logs, pursuant to 10 CFR 73.71, and found that
In February 1988, the licensee performed both an Operational
                                  nearly 93% of the logged security incidents are attributable tc
Readiness Review (NSB/CA 88-01) and its annual Quality Assurance
                                  failed alarms, cameras, computers and coded-key card readers.
Audit (SSA-88-06) which resulted in the identification of
                                  The same assessment noted a minor reduction in the number of
persistent hardware and equipment inadequacies and the continued
                                  compensatory measures, due to the correct prioritization of work
dependence on compensatory measures.
                                  requests and a relatively short turnaround time for repair of
While no Conditions
                                  security equipment. It is noted that the licensee-identified
Adverse to Quality were identified, the Audit concluded that
                                  violations for officers being found inattentive to duty have a
some of the equipment was obsolete and restricted the
effectiveness of the security program.
NRC has ascessed the
Safeguards Event Logs, pursuant to 10 CFR 73.71, and found that
nearly 93% of the logged security incidents are attributable tc
failed alarms, cameras, computers and coded-key card readers.
The same assessment noted a minor reduction in the number of
compensatory measures, due to the correct prioritization of work
requests and a relatively short turnaround time for repair of
security equipment.
It is noted that the licensee-identified
,
,
violations for officers being found inattentive to duty have a
'
'
                                  direct relationship to the extensive use of compensatory
direct relationship to the extensive use of compensatory
                                  measures.   Much of the security equipment was poorly designed
measures.
                                  and installed, and has over the years fallen into a state of
Much of the security equipment was poorly designed
                                  disrepair such that replacement parts are not always readily
and installed, and has over the years fallen into a state of
                                  available.     The NRC found several examples where vendor
disrepair such that replacement parts are not always readily
                                  furnished parts needed to be extensively altered before being
available.
The NRC found several examples where vendor
furnished parts needed to be extensively altered before being
!
!
      ..
..
              .
.
                  _ - _______ __                 _
_ - _______ __
                                                                                                                        l
_
l


                                                                                          _ _ _ _ _ _ -
_ _ _ _ _ _ -
                                                                                                        ..
..
        '
'
    .
.
    ..
..
  -
41
                                      41
-
            used in the current security system.       In the interim, the
used in the current security system.
            licensee implemented appropriate compensatory measures.
In the interim, the
            At the Corporate level, the licensee continued to experience
licensee implemented appropriate compensatory measures.
            attrition at its senior security management level. During this
At the Corporate level, the licensee continued to experience
            ' assessment period the ninth manager in the last 10 years re-
attrition at its senior security management level. During this
          -
' assessment period the ninth manager in the last 10 years re-
            signed.   As a result of this continued turnover, numerous
signed.
            assessments, evaluations and studies have been conducted with
As a result of this continued turnover, numerous
            correspondingly few corrective action programs reaching fruition.
-
            After appointment of the most recent and current managers the
assessments, evaluations and studies have been conducted with
            NRC can now begin to see significant progress made on several
correspondingly few corrective action programs reaching fruition.
            old projects, some of which have been successfully completed.
After appointment of the most recent and current managers the
              In July 1988, the licensee finalized the reorganization of its
NRC can now begin to see significant progress made on several
            Corporate Nuclear Security Services Branch so that there now
old projects, some of which have been successfully completed.
            exists a centralized (and accountable) management system.
In July 1988, the licensee finalized the reorganization of its
            Within this Branch there is a security compliance section, a
Corporate Nuclear Security Services Branch so that there now
            consolidated plant access and screening unit, a separate section
exists a centralized (and accountable) management system.
            responsible for equipment upgrade and another section tasked
Within this Branch there is a security compliance section, a
            with plans and procedures. A key element of the Branch is a
consolidated plant access and screening unit, a separate section
            Safeguards Information Network which will computerize all site
responsible for equipment upgrade and another section tasked
              and corporate data. Another indication of improvement is the
with plans and procedures.
            upgrading of security training and increased tactical exercises,
A key element of the Branch is a
            Multiple Integrated Laser Engagement System (MILES) is available
Safeguards Information Network which will computerize all site
              to add to the realism of these drills. The licensee's canine
and corporate data.
              corp is recogniz.ed by other federal and state agencies for its
Another indication of improvement is the
              expertise in detecting contraband.
upgrading of security training and increased tactical exercises,
            At the site level, there exists a direct management matrix from
Multiple Integrated Laser Engagement System (MILES) is available
              the Site Security Managcr to the Corporate Manager of Protective
to add to the realism of these drills.
              Services within the Nuclear Power Group. The Site Director and
The licensee's canine
              the Plant Manager have been instrumental in c'edicating site
corp is recogniz.ed by other federal and state agencies for its
L            support to reduce the number of security compensatory measures.
expertise in detecting contraband.
              While technically there is a matrixed relationship between the
At the site level, there exists a direct management matrix from
              site and its security organization there is a very strong
the Site Security Managcr to the Corporate Manager of Protective
              matrixed interface.
Services within the Nuclear Power Group. The Site Director and
              Changu to Physical Security, Contingency, and Cuard Training
the Plant Manager have been instrumental in c'edicating site
              and Qualification Plans were generally well-prepared and
support to reduce the number of security compensatory measures.
              coordinated, with one exceptior.. The licensee withdrew one
L
              revision to the Physical Security Plan when it was discovered to
While technically there is a matrixed relationship between the
              contain a number of errors and omissions. The licensee has been
site and its security organization there is a very strong
              very responsive to questions and concerns raised on licensing
matrixed interface.
              submittals.
Changu to Physical Security, Contingency, and Cuard Training
              The NRC has noticed an improvement in the quality of the
and Qualification Plans were generally well-prepared and
              security staff while the size of the staff has been reduced.
coordinated, with one exceptior..
              This is evidenced in such key elements as training and
The licensee withdrew one
              procedural knowledge.     There now appears to be a premeditated
revision to the Physical Security Plan when it was discovered to
              implementation of the security program, as opposed to a reactive
contain a number of errors and omissions. The licensee has been
              security program.
very responsive to questions and concerns raised on licensing
submittals.
The NRC has noticed an improvement in the quality of the
security staff while the size of the staff has been reduced.
This is evidenced in such key elements as training and
procedural knowledge.
There now appears to be a premeditated
implementation of the security program, as opposed to a reactive
security program.
l
l
                                                                  ___- ______-_____-__-_ - _ ~
___- ______-_____-__-_ - _ ~


          .                       .
.
      '                       *
.
  ..t
'
    .
*
  -
..t
                                                                                                              42
.
p                                                                                                                                ,
42
                                                                                    No violations were identified:
-
                                                                                                                                                .
p
!                                                                               2.   Performance Rating:
,
No violations were identified:
.
!
2.
Performance Rating:
l'
l'
                                                                                    Category 2
Category 2
                                                                                3.   Recommendations:
3.
                                                                                    The Board recommends that the licensee review it's security
Recommendations:
                                                                                    upgrade priorities at all three facilities to ensure that the
The Board recommends that the licensee review it's security
                                                                                    Sequoyah security program continues to reduce its long term
upgrade priorities at all three facilities to ensure that the
                                                                                    reliance on compensatory measures in lieu of reliable security
Sequoyah security program continues to reduce its long term
                                                                                    equipment and systems.
reliance on compensatory measures in lieu of reliable security
                                                                        F.     Engineering / Technical Support
equipment and systems.
                                                                                1.   Analysis
F.
                                                                                    NRC involvement in the engineering and technical support area
Engineering / Technical Support
                                                                                    was more comprehensive than normally applied to licensee
1.
                                                                                    activities.   This resulted from interactions between NRC OSP
Analysis
                                                                                    and the licensee necessary to achieve acceptable engineering
NRC involvement in the engineering and technical support area
                                                                                    resolutions as described previously in the summary section and
was more comprehensive than normally applied to licensee
                                                                                    the technical complexity of many of the engineering issues.
activities.
                                                                                    The Engineering / Technical Support functional crea eccresses the
This resulted from interactions between NRC OSP
                                                                                    adequacy of the technical and engineering support for all plant
and the licensee necessary to achieve acceptable engineering
                                                                                    activities.   To determine the adequacy of the suppcrt previded,
resolutions as described previously in the summary section and
                                                                                    specific attention was given to assurance of quality, includir.g
the technical complexity of many of the engineering issues.
                                                                                    management involvement and control, the identification and
The Engineering / Technical Support functional crea eccresses the
                                                                                    approach to resolution of technical issues, respersiveness to
adequacy of the technical and engineering support for all plant
                                                                                    NRC initiatives,     enforcement history,     opera tior,al and
activities.
                                                                                    construction events, staffing, and effectiveness cf training,
To determine the adequacy of the suppcrt previded,
,                                                                                    and qualification. This area includes all licensee activities
specific attention was given to assurance of quality, includir.g
                                                                                    associated with design baseline evaluation irrplcr.:entation in
management involvement and control, the identification and
                                                                                    terms of Sequoyah plant modifications, engineering and
approach to resolution of technical issues, respersiveness to
                                                                                    technical support provided for operations, maintenance,
NRC initiatives,
                                                                                    surveillance,   training,   procurement,   and   configuration,
enforcement history,
                                                                                    management.     This evaluation was based on Sequoyah site
opera tior,al
                                                                                    inspections conducted by the NRC staff in the above areas and on
and
                                                                                    licensee technical submittals reviewed by the staff containir.g
construction events, staffing, and effectiveness cf training,
                                                                                    engineering evaluations . supporting the Sequoyah Nuclear
and qualification.
                                                                                    Performance Plan (SNPP).           .
This area includes all licensee activities
                                                                                      Inadequacies during the basis period were in the areas of design
,
                                                                                    analysis, modification control, engineering docume nta tion ,
associated with design baseline evaluation irrplcr.:entation in
                                                                                    design basis utilization, and design verification. In order to
terms of Sequoyah plant modifications, engineering and
                                                                                    correct these weaknesses, TVA senior management increased their
technical support provided for operations, maintenance,
                                                                                    involvement and control during this assessment period to improve
surveillance,
                                                                                      the quality of engineering support.     TVA nanagement involvement
training,
                                                                                    was demonstrated through issues including; the Replacement Items
procurement,
                                                                                    Prngram, in which TVA Corporate and Sequoyah management were
and
                                                                                    greatly involved in the program to ensure immediate and effective
configuration,
                                                                                    corrective action; the issuance and use of procedures in the
management.
                                                                                    civil / structural area, including pipe supports and restraints;
This evaluation was based on Sequoyah site
        ___ _ _ __ - _ - _ _ - _ - _ - _ _ _ _ _ _ - _ _ _ _ _ _ _ _ _ _ - _ .
inspections conducted by the NRC staff in the above areas and on
licensee technical submittals reviewed by the staff containir.g
engineering evaluations . supporting the Sequoyah Nuclear
Performance Plan (SNPP).
.
Inadequacies during the basis period were in the areas of design
analysis, modification control, engineering docume nta tion ,
design basis utilization, and design verification.
In order to
correct these weaknesses, TVA senior management increased their
involvement and control during this assessment period to improve
the quality of engineering support.
TVA nanagement involvement
was demonstrated through issues including; the Replacement Items
Prngram, in which TVA Corporate and Sequoyah management were
greatly involved in the program to ensure immediate and effective
corrective action; the issuance and use of procedures in the
civil / structural area, including pipe supports and restraints;
___ _ _ __ - _ - _ _ - _ - _ - _ _ _ _ _ _ - _ _ _ _ _ _ _ _ _ _ - _ .


                - _   -   _             _   -                 _
- _
                                                                                  _
-
k   g
_
              ;
_
                    ,
-
                              -
_
        ..
_
                        '
k
            '
-
      .                                                 .43
;
                                'the drawing: control' process,.which is considered .now to be .of             ~
g
Io                           ' high quality and. accuracy; and the procedures .for control: of
,
I                               thermal expansion tests. The procedures used for the thermal
..
                                expansion tests were well defined and explicit, demonstrating
'
                                evidence of prior planning with a proper assignment of
.43
                                priorities.
'
  ,
.
                                In . response to ' concerns expressed by the NRC, TVA revised
'the drawing: control' process,.which is considered .now to be .of
                                Sequoyah's snubber surveillance program procedures, resulting in
~
                                a- more conservative selection.of the number of snubbers to be
Io
                                tested upon occurrence of test failures.
' high quality and. accuracy; and the procedures .for control: of
                            -TVA DNE continued the control of the EQ activities as had been
I
                                established in 1986 and 1987. During thisLassessment period,
thermal expansion tests.
                                Sequoyah'transitioned from a separate dedicated EQ' organization
The procedures used for the thermal
                                to a matrix organization within the site DNE organization. This
expansion tests were well defined and explicit, demonstrating
                                transition appeared to occur without interruption or degradation
evidence of prior planning with a proper assignment of
                                of the quality of DriE support to the plant.                       Engineering
priorities.
                                decisions were made at appropriate levels.         This is'a clear
,
                            ; example' of TVA . DNE management involvement and control in
In . response to ' concerns expressed by the NRC, TVA revised
                                assuring quality.
Sequoyah's snubber surveillance program procedures, resulting in
                                Other issues in which DNE management oversight and involvement
a- more conservative selection.of the number of snubbers to be
                                was 'strongly prevalent included DNE representation during the
tested upon occurrence of test failures.
                                morning and outage planning meetings, the initiation cf a duty
-TVA DNE continued the control of the EQ activities as had been
          .                    DNE manager for weekend and back shift engineering support for
established in 1986 and 1987.
    '
During thisLassessment period,
                                Op.erations, and the direct management involvement in the
Sequoyah'transitioned from a separate dedicated EQ' organization
                                organization.and allocation of resources for the P,estart Test       -
to a matrix organization within the site DNE organization. This
                                Program.
transition appeared to occur without interruption or degradation
                                TVA DNE management, hoviever, has not been adequately involved to
of the quality of DriE support to the plant.
                                ensure quality in all cases.    S                                                        1
Engineering
                                provided in Generic Letter (GL)         specifically,
decisions were made at appropriate levels.
                                                                      86-10, for spuriousthe              staff guidance
This is'a clear
                                                                                                        actuations
; example' of TVA . DNE management involvement and control in
                                from high-impedance faults had not been followed by TVA.
assuring quality.
                                Similar problems with 'the implementation and ' applicability of
Other issues in which DNE management oversight and involvement
                                other portions of GL 86-10 had been previously discussed with
was 'strongly prevalent included DNE representation during the
                                the licensee early in the assessment period. This instance
morning and outage planning meetings, the initiation cf a duty
                                indicated a reliance of the licensee on the NRC to establish an                             ;
DNE manager for weekend and back shift engineering support for
                                adequate scope and content for this generic letter with respect                           j
.
                                to the extent of applicability and indicated a lack of                                   ,
Op.erations, and the direct management involvement in the
                                                                                                                          !
'
                                responsiveness to this NRC initiative.
organization.and allocation of resources for the P,estart Test
                                                                                                                          '
Program.
                                TVA did not follow their design commitments made to the NRC
-
                                involving criteria for pipe supports and piping analyses. These                           i
TVA DNE management, hoviever, has not been adequately involved to
                                cases indicated a lack of management involvement in the
provided in Generic Letter (GL) specifically, the staff guidance
                                activities they supervise and a lack of quality verification for                           I
ensure quality in all cases.
                                commitments made to the NRC.       ,
S
                                TVA experienced problems in engineering documentation adequacy
1
                                and in the backlog of open plant change packages. For example,
86-10, for spurious actuations
                                TVA did not properly document changes to the Emergency Diesel
from high-impedance faults had not been followed by TVA.
                                                                                                                          )
Similar problems with 'the implementation and ' applicability of
                                                                                                                            i
other portions of GL 86-10 had been previously discussed with
                                                                                                                        .
the licensee early in the assessment period.
                                                                                    __- ___ _ _ - _
This instance
indicated a reliance of the licensee on the NRC to establish an
;
adequate scope and content for this generic letter with respect
j
to the extent of applicability and indicated a lack of
,
!
responsiveness to this NRC initiative.
'
TVA did not follow their design commitments made to the NRC
involving criteria for pipe supports and piping analyses. These
i
cases indicated a lack of management involvement in the
activities they supervise and a lack of quality verification for
I
commitments made to the NRC.
,
TVA experienced problems in engineering documentation adequacy
)
and in the backlog of open plant change packages.
For example,
TVA did not properly document changes to the Emergency Diesel
i
__- ___ _ _ - _
.


,                                                                                       _               _   _
,
                                                                                                                __ _ _ - _ _ - _ - _ - -
_
      g     '
_
                          '
_
          ..                                                                                               .
__ _ _ - _ _ - _ - _ - -
        .       #                                                  44
g
                              Generator (EDG) 2B-B load analysis (SQN-E3-002) from Rev'ision 7,
'
                              which was used as the' basis for Unit 2 restart, to Revision 10,
'
                              in which all EDGs were analyzed. for Unit 1~ restart. Revision
..
                              10 which documented that EDG 28-B had reduced diesel generator
.
                              loading,~ 1acked complete information and required additional
44
                              supporting data to explain the leading changes. 'Furthermore,
#
                              the summary letter of EDG load analysis dated August 11, 1988.
.
                              contained three incorrect-numbers, only'_one of which was later
Generator (EDG) 2B-B load analysis (SQN-E3-002) from Rev'ision 7,
                              identified by TVA.                   NRC staff discussions with modification
which was used as the' basis for Unit 2 restart, to Revision 10,
                            - personnel revealed there were approximately 1300 engineering
in which all EDGs were analyzed. for Unit 1~ restart.
                              design change workplans: remaining open, some dating back to
Revision
                              1980. All required physical work was completed on these work-
10 which documented that EDG 28-B had reduced diesel generator
                              plans prior to plant startup, however, the workplans were
loading,~ 1acked complete information and required additional
                              'left open!for various reasor.s. These problems indicate lack of
supporting data to explain the leading changes.
                              quality, verification for submittals made to the NRC and a lack-of
'Furthermore,
                              management'_invoiva ent.
the summary letter of EDG load analysis dated August 11, 1988.
                              The approaches taken by the site end corporate engineering-
contained three incorrect-numbers, only'_one of which was later
                              staffs to resolve technical issues from a safety standpoint were
identified by TVA.
                              adequate with improvement shcwn during the assessment period.
NRC staff discussions with modification
                              For example, in the civil / structural area, the staff reviewed
- personnel revealed there were approximately 1300 engineering
                            - TVA's submittals for justifying the adequacy _of Interim (or.-
design change workplans: remaining open, some dating back to
                              Restart) Criteria and design calculations for a. field erected
1980.
                                                                                ~
All required physical work was completed on these work-
                              tank, cable tray supports, pipe supports, conduit and supports,
plans prior to plant startup, however, the workplans were
                              ERCU pipe access cells, the ERCW pump station, masonry walls,
'left open!for various reasor.s. These problems indicate lack of
                              .the steel . containment vessel, equipment supports and miscel-                                             .
quality, verification for submittals made to the NRC and a lack-of
                              laneous civil / structural issues, and found that the engineering
management'_invoiva ent.
                              records and design calculations were generally complete end
The approaches taken by the site end corporate engineering-
                              documented. However, as a result of NRC reviews, some of the
staffs to resolve technical issues from a safety standpoint were
                              design calculations were regenerated two cr three times by TVA
adequate with improvement shcwn during the assessment period.
                              before lVA was able to r'eet and implement restart requirement
For example, in the civil / structural area, the staff reviewed
                              design criteria which was acceptable to the NRC. The evaluation
- TVA's submittals for justifying the adequacy _of Interim (or.-
                                results for' the issues' iden:1fied were' reascnable, logical and
Restart) Criteria and design calculations for a. field erected
                                                                    -
~
                              net the Sequoyah restart requirements. In the area of pipe
tank, cable tray supports, pipe supports, conduit and supports,
                              supports, cable tray supports, pipe restraints and equipment
ERCU pipe access cells, the ERCW pump station, masonry walls,
                              supports, staff review ano evaluation found that there was a
.the steel . containment vessel, equipment supports and miscel-
                              defined set of procedures for the control of engineering
.
                              activities.             It was concluded that engineering records were
laneous civil / structural issues, and found that the engineering
                                available, relatively easy to access and were clear. Minor
records and design calculations were generally complete end
                              errors were found in some of the specific calculation packages
documented.
                                reviewed, however, the general assessment was that TVA had
However, as a result of NRC reviews, some of the
                                improved the quality of the results of the engineering and
design calculations were regenerated two cr three times by TVA
                                technical support groups.
before lVA was able to r'eet and implement restart requirement
                              TVA engineering personnel were found to have an understanding of                                             !
design criteria which was acceptable to the NRC. The evaluation
                                the issues involved when evaluating changes to the facility.
results for' the issues' iden:1fied were' reascnable, logical and
                              The staff audited the licensee's report required under 10 CFR
-
      '
net the Sequoyah restart requirements.
                                50.59 supporting the seismic qualification of the interim and
In the area of pipe
                                final designs associated with the component cooling water (CCW)
supports, cable tray supports, pipe restraints and equipment
                                heat exchanger replacement and associated piping modifications.
supports, staff review ano evaluation found that there was a
- _-__         _   __ _ -           _ _ _ - _ - _ _ _       - _ -     _ - _ _   - _ _ .   - - _ ._ _ _ _
defined set of procedures for the control of engineering
activities.
It was concluded that engineering records were
available, relatively easy to access and were clear.
Minor
errors were found in some of the specific calculation packages
reviewed, however, the general assessment was that TVA had
improved the quality of the results of the engineering and
technical support groups.
TVA engineering personnel were found to have an understanding of
!
the issues involved when evaluating changes to the facility.
The staff audited the licensee's report required under 10 CFR
50.59 supporting the seismic qualification of the interim and
'
final designs associated with the component cooling water (CCW)
heat exchanger replacement and associated piping modifications.
- _-__
_
__ _ -
_ _ _ - _ - _ _ _
- _ -
_ - _ _
- _ _ .
- - _
._ _ _ _


      ,                                                   . - - _ _ _ _ - _ - - - - - _ _
,
    d
. - -
  .
_ _ _
-                                 45
_ - _ - - - - - _ _
        The detailed analyses provided to the staff exhibited a
d
        comprehensive evaluation of the CCW system to justify continued
.
        operation of Unit I while the piping modifications were being
45
        implemented.     The engineering records were extensively
-
        documented and readily available for staff audit. The licensee
The detailed analyses provided to the staff exhibited a
        exhibited a thorough understanding of the technical analyses and
comprehensive evaluation of the CCW system to justify continued
        clearly explained the rationale for allowing continued operation
operation of Unit I while the piping modifications were being
        of Unit 1 during the CCW heat exchanger changeout.
implemented.
        Further examples of adequate TVA engineering reviews included
The engineering records were extensively
        the piping thermal expansion test program which demonstrated a
documented and readily available for staff audit. The licensee
        sound and thorough approach to identifying potential inter-
exhibited a thorough understanding of the technical analyses and
        ference to piping thermal growth as a result of implementation
clearly explained the rationale for allowing continued operation
        of plant modifications.     Also, TVA's response to the staff's
of Unit 1 during the CCW heat exchanger changeout.
        concerns regarding potential damage to the containment during
Further examples of adequate TVA engineering reviews included
        the Sequoyah extended shutdown period demonstrated a sound
the piping thermal expansion test program which demonstrated a
        approach to resolving the staff's concerns.
sound and thorough approach to identifying potential inter-
        However, in several instances during the assessment period, TVA
ference to piping thermal growth as a result of implementation
        actions indicated an inconsistency in the thoroughness of
of plant modifications.
        technical resolutions and a lack of attention to detail.
Also, TVA's response to the staff's
        Examples of weak technical resolutions and lack of thoroughness
concerns regarding potential damage to the containment during
        included TVA's initial cable testing program, EDG voltage
the Sequoyah extended shutdown period demonstrated a sound
        analysis (SQN-E3-011, Revision 2,) and a proposed TS change
approach to resolving the staff's concerns.
        which applied to the Turbine Driven Auxiliary Feedwater Pump.
However, in several instances during the assessment period, TVA
        (TDAFWP).     TVA demonstrated a general understanding of the
actions indicated an inconsistency in the thoroughness of
        safety issues' involved, however, the engineering analysis
technical resolutions and a lack of attention to detail.
        accompanying these issues did not reflect an indepth review of
Examples of weak technical resolutions and lack of thoroughness
        all applicable safety aspects. The DNE effort supporting the
included TVA's initial cable testing program, EDG voltage
        Sequoyah Unit 2 pressurizer safety valve steam trim / leakage
analysis (SQN-E3-011, Revision 2,) and a proposed TS change
        resolution was another exmple of a lack of effective DNE action
which applied to the Turbine Driven Auxiliary Feedwater Pump.
        to resolve plant problems.
(TDAFWP).
        The staff audited the licensee's modification to correct a
TVA demonstrated a general understanding of the
        deficiency in the teismic qualification of Bailey Meter elec-
safety issues' involved, however, the engineering analysis
        trical_ instrumentation cabinets involving the use of aircraft
accompanying these issues did not reflect an indepth review of
        cable. The staff found the licensee's modification to be                           ;
all applicable safety aspects.
        unacceptable.     The licensee did not demonstrate an under-                     i
The DNE effort supporting the
        standing of the seismic qualification requirements for the                         l
Sequoyah Unit 2 pressurizer safety valve steam trim / leakage
        Bailey Meter cabinets and thus its fix, using aircraft cable,                     j
resolution was another exmple of a lack of effective DNE action
        was not sound. In addition, only after the modification using                     i
to resolve plant problems.
        the aircraft cable was found to be unacceptable, did the                           f
The staff audited the licensee's modification to correct a
        licensee establish that the electrical instrumentation was not
deficiency in the teismic qualification of Bailey Meter elec-
        required for safe shutdown.
trical_ instrumentation cabinets involving the use of aircraft
                                                                                          '
cable.
        While the level of cooperation between DNE and plant personnel
The staff found the licensee's modification to be
        has substantially improved, the technical adequacy of the
;
        engineering support has not been of a consistently high level.
unacceptable.
        While progress over the assessment period was evident, errors
The licensee did not demonstrate an under-
        and incomplete evaluations have continued.
i
                                  -
standing of the seismic qualification requirements for the
Bailey Meter cabinets and thus its fix, using aircraft cable,
j
was not sound.
In addition, only after the modification using
i
the aircraft cable was found to be unacceptable, did the
f
licensee establish that the electrical instrumentation was not
required for safe shutdown.
'
While the level of cooperation between DNE and plant personnel
has substantially improved, the technical adequacy of the
engineering support has not been of a consistently high level.
While progress over the assessment period was evident, errors
and incomplete evaluations have continued.
-


                                                                                            _ _ _ _   _ _ _ - _ __ _ _
_ _ _ _
    .;             D
_ _ _ - _
        ._-
__ _
    -
_
g                                                           46
D
                                ' During the assessment period, tha licensee generally responded
.;
                                  well to NRC initiatives. While NRC'had to. insist on cable type
._-
                                                                              -
46
                                                                                                                          '
-
                                  testing, TVA has since been responsive in all remaining areas of                    H  '
g
                                  the cable testing program. . Other examples of TVA's responsive-
' During the assessment period, tha licensee generally responded
                                  ness .were demonstrated in the ' area of procurement. In.a few -                      ;
well to NRC initiatives.
                                  Leases (e.g. molded case circuit. breakers) Sequoyah engineering-                      l
While NRC'had to. insist on cable type
                                  staff exceeded reporting requirements to the NRC with respect to                      l
                                  reporting the s_ cope of problems. ThisJ assisted the NHC in                          !
                                  providing up-to-date. guidance to other licensees..'In the area                        !
  >                              'of fire protection,- responses to NRC requests have generally -
                                  been timely as well;as thorough except for certain provisions of
                                  GL 86-10.    An exception was_in the area'of~ establishing welding                    >
                                  inspector certification where records were not complete nor well
                                  maintained and corrective action was not timely. Other respon-                        i
                                                                                                                          '
                                  sive efforts worth noting include the timely corrective action
                                  taken for problems identified during the pre-operational thermal                      j
                                  expansion- test program.    These efforts represented timely                          ;
                                  corrective action implementation for an NRC initiative which                          ;
                                  went beyond minimum NRC requirements and, with TVA's proper                          i
                                  completion - of = the test program, significantly enhanced the
                                  reliability of the Sequoyah piping systems.
                                  During the assessment period two violations were issued in the                        !
                                  Engineering / Technical Support area.  The first violation was for                  '
                                  failure to take adequate corrective action and follow procedures                      ;
                                  relative to dedication of commercial grade items for use in                          ;
                                  safety-related applications. While NRC had observed improve-                          l
                                  ments in TVA's procurement of purchased parts due to previous                        i
                                  corrective actions, the inspection determined that Sequoyah was
                                  still procuring commercial grade parts without adequate                            H
                                  dedication of the parts for use in safety-related applications.                      j
                                  The second violation documented that TVA did not have hydraulic                    -j
      +                          . and thermal design calculations for the containment spray                            l
                                  system, which estcalished the design basis for the pressure ard
                                    temperature bourcaries.    Corrective actions for both of the
                                  above violations have been implemented and were determined
                                    edequate.
                                  Operational and construction events which involved TVA                                )
                                    engineering have been properly reported to the staff via the
                                    Licensee Event Reporting system. Engineering support for these                      ,
                                    occasions was adequate to support both proposed and implemented                      j
'
'
                                    corrective actions.                                                                 !
-
                                                                                                                          l
testing, TVA has since been responsive in all remaining areas of
                                    TVA staffing levels in the engineering / technical support area,
H
                                    including management, were adequate. Position identifications                       I
'
                                    and definitions of authority and responsibility were well
the cable testing program. . Other examples of TVA's responsive-
                                    established and managed during the assessment period.           In the
ness .were demonstrated in the ' area of procurement.
                                    civil / structural engineering area, the items that required
In.a few -
                                    resolution by TVA engineering from the NRC's Safety System                           l
;
            _ _ _ _ - - _ _ _ __             _                                                                         )
Leases (e.g. molded case circuit. breakers) Sequoyah engineering-
l
l
staff exceeded reporting requirements to the NRC with respect to
reporting the s_ cope of problems. ThisJ assisted the NHC in
!
providing up-to-date. guidance to other licensees..'In the area
!
'of fire protection,- responses to NRC requests have generally -
>
been timely as well;as thorough except for certain provisions of
GL 86-10.
An exception was_in the area'of~ establishing welding
>
inspector certification where records were not complete nor well
maintained and corrective action was not timely.
Other respon-
i
'
sive efforts worth noting include the timely corrective action
taken for problems identified during the pre-operational thermal
j
expansion- test program.
These efforts represented timely
;
corrective action implementation for an NRC initiative which
;
i
went beyond minimum NRC requirements and, with TVA's proper
completion - of = the test program, significantly enhanced the
reliability of the Sequoyah piping systems.
During the assessment period two violations were issued in the
!
'
Engineering / Technical Support area.
The first violation was for
failure to take adequate corrective action and follow procedures
;
relative to dedication of commercial grade items for use in
;
safety-related applications.
While NRC had observed improve-
l
i
ments in TVA's procurement of purchased parts due to previous
corrective actions, the inspection determined that Sequoyah was
still procuring commercial grade parts without adequate
H
dedication of the parts for use in safety-related applications.
j
The second violation documented that TVA did not have hydraulic
-j
. and thermal design calculations for the containment spray
l
+
system, which estcalished the design basis for the pressure ard
temperature bourcaries.
Corrective actions for both of the
above violations have been implemented and were determined
edequate.
Operational and construction events which involved TVA
)
engineering have been properly reported to the staff via the
Licensee Event Reporting system.
Engineering support for these
,
occasions was adequate to support both proposed and implemented
j
corrective actions.
!
l
'
TVA staffing levels in the engineering / technical support area,
including management, were adequate.
Position identifications
I
and definitions of authority and responsibility were well
established and managed during the assessment period.
In the
civil / structural engineering area, the items that required
resolution by TVA engineering from the NRC's Safety System
l
_ _ _ _ - - _ _ _ __
_
)


                                                                              1
1
      4
j
. .;                                                                         j
4
    .
. .;
.                                   47                                        .
.
                                >
47
                                                                              (
.
                                                                              '
.
          Quality Evaluation, were in some instances delayed because of       '
>
          lack of available staff.     However, this was noted as an
'
          exception rather than the norm.'
Quality Evaluation, were in some instances delayed because of
                                                                              9
'
          The effectiveness of TVA's training and qualification programs
lack of available staff.
          in engineering and technical support has generally been adequate
However, this was noted as an
          with a few exceptions. Lack of adequate training was a major
exception rather than the norm.'
          cause of a violation in the procurement area.       A lack of
9
          adequate training in administrative procedures was found to         j
The effectiveness of TVA's training and qualification programs
          be a major contributing factor in ISI training and documentation   j
in engineering and technical support has generally been adequate
          problems and in the reluctance by the ISI group members who
with a few exceptions.
          performed radiography on welds to follow administrative
Lack of adequate training was a major
          requirements for procedure changes.       These events were
cause of a violation in the procurement area.
          inconsistent with the observed results of training for other TVA
A lack of
          organizations (e.g. plant modification training, maintenance
adequate training in administrative procedures was found to
          craft training, and Shif t Technical Advisor and Operator
j
          training). The pre-operational thermal expansion test program
be a major contributing factor in ISI training and documentation
          engineers were noted as being well trained ano qualified for the   i
j
          performance of their required duties. In general, the training
problems and in the reluctance by the ISI group members who
          and qualification programs contributed to an adequate under-
performed radiography on welds to follow administrative
          standing of work and general adherence to procedures. The number
requirements for procedure changes.
          of exceptions were acceptable. Management of the training and
These events were
          qualification program within the ISI area was inadequate in that
inconsistent with the observed results of training for other TVA
          adherence to administrative procedures was not enforced.
organizations (e.g. plant modification training, maintenance
          Two violations were identified:
craft training, and Shif t Technical Advisor and Operator
          a.   Severity Lesel IV violation for failure to take adequate
training).
                corrective acticn and follow procedures relative to
The pre-operational thermal expansion test program
                dedication of commercial grade items for use in safety-
engineers were noted as being well trained ano qualified for the
                related applications. (88-07-01)
i
          b.   Severity Level IV violation for failure to hase hydraulic
performance of their required duties.
                and thermal design calculations for the cont 6inment spray
In general, the training
                system. (88-29-01)
and qualification programs contributed to an adequate under-
        2. Performance Rating:
standing of work and general adherence to procedures. The number
          Category: 3 Improving
of exceptions were acceptable.
        3. Recommendations:
Management of the training and
          The Board is encouraged by the initiative and efforts expendeo
qualification program within the ISI area was inadequate in that
          by TVA to improve the quality and effectiveness of its             ,
adherence to administrative procedures was not enforced.
          engineering suppcrt for the Sequoyah Nuclear Plant.     The Board
Two violations were identified:
          recognizes that a significant amount of complex engineering work   '
a.
          was completed. Since considerable NRC effort and input was
Severity Lesel IV violation for failure to take adequate
          needed to obtain acceptable engineering resolutions, the 00ard
corrective acticn and follow procedures relative to
          concluded that TVA has not yet demonstrated independent
dedication of commercial grade items for use in safety-
          performance at a level greater than that necessary to meet
related applications. (88-07-01)
          minimum regulatory requirements.     The Ecard recoiserds that
b.
                                                                              !
Severity Level IV violation for failure to hase hydraulic
                                                                              ;
and thermal design calculations for the cont 6inment spray
system. (88-29-01)
2.
Performance Rating:
Category: 3 Improving
3.
Recommendations:
The Board is encouraged by the initiative and efforts expendeo
by TVA to improve the quality and effectiveness of its
engineering suppcrt for the Sequoyah Nuclear Plant.
The Board
,
recognizes that a significant amount of complex engineering work
was completed.
Since considerable NRC effort and input was
'
needed to obtain acceptable engineering resolutions, the 00ard
concluded that TVA has not yet demonstrated independent
performance at a level greater than that necessary to meet
minimum regulatory requirements.
The Ecard recoiserds that
!
;


_ - .
_ - .
            .                                      .
.
        ,
,
          .
.
                                                                                                            j
j
      _
.
                                                48                                                           )
48
                                                                                                            i
)
                      management attention to this area continue, that those long term                     j
_
                      commitments made ' to assure continued improvement after the                           '
i
                      initial restart of both units be completed as scheduled, and
management attention to this area continue, that those long term
                      that adequate long term staffing and funding be maintained to                       i,
j
                                                                                                            '
commitments made ' to assure continued improvement after the
                      support completion of the long term commitments.
'
              G. S_afety Assessment / Quality Verification
initial restart of both units be completed as scheduled, and
                1.   Analysis
that adequate long term staffing and funding be maintained to
                      The area of Safety Assessment / Quality Verification included
i,
                      quality assurance and the corrective action process, safety
'
                      committees, the 10 CFR 50.59 safety evaluation program, event
support completion of the long term commitments.
                      reporting and root cause assessment, the employee concerns
G.
                      program, licensing activities, and corporate support for quality
S_afety Assessment / Quality Verification
                      verification.     The most significant improvement *las i~n the
1.
                      corrective action program which is now functioning adequately.
Analysis
                      Improvements were ncted in safety committee performance and root
The area of Safety Assessment / Quality Verification included
                      cause assessment.     Weaknesses were noted in the 10 CFR 50.59
quality assurance and the corrective action process, safety
                      safety evaluation program.
committees, the 10 CFR 50.59 safety evaluation program, event
                      While both site and corporate management were involved in the CA
reporting and root cause assessment, the employee concerns
                      area and the policies were adequately stated, NRC inspections
program, licensing activities, and corporate support for quality
                      and other NRC staff reviews and evaluations indicated that all
verification.
                      new policies were not fully understood by Seoucyah personnel.
The most significant improvement *las i~n the
                      Problems continued to exist during the early part of the rating
corrective action program which is now functioning adequately.
                      period in the corrective action process and cdequate corrective
Improvements were ncted in safety committee performance and root
                      action was occasionally not effective resulting in repetitive
cause assessment.
                      CAQRs.     In addition, CAQR resolutions were sometimes delayed.
Weaknesses were noted in the 10 CFR 50.59
                      Changes to the QA topical report are requirea to be submitted to
safety evaluation program.
                      the NRC at least yearly. TVA made several extension requests
While both site and corporate management were involved in the CA
                      for submittal of changes indicating a slow approval process end
area and the policies were adequately stated, NRC inspections
                      a reliance on the NRC to establish an adequate time frame for
and other NRC staff reviews and evaluations indicated that all
                      submittal. * While the violations that occurred during the
new policies were not fully understood by Seoucyah personnel.
                      assessment period have not been directly related to the QA
Problems continued to exist during the early part of the rating
                      program, they have involved failure to follow procedures or
period in the corrective action process and cdequate corrective
                      failure to take adequate corrective action.
action was occasionally not effective resulting in repetitive
                      Key positions in the QA department were identified and
CAQRs.
                      authorities and responsibilities were well defined. The staff
In addition, CAQR resolutions were sometimes delayed.
                      expertise level was considered excellent.     Trcining contributed
Changes to the QA topical report are requirea to be submitted to
                      to an adequate understanding of the QA prcgram.
the NRC at least yearly.
                      The licensee continued the implementation of the CAQR program
TVA made several extension requests
                      which was established during the basis pericd.       Early in the                   '
for submittal of changes indicating a slow approval process end
                      assessment period CAQR reviews indicated weaknesses in opera-
a reliance on the NRC to establish an adequate time frame for
                      bility and significance determinations, reviewer and management
submittal. * While the violations that occurred during the
                      training, timeliness, documentation, and auditability of re-
assessment period have not been directly related to the QA
                      cores. The Sequoyah Site Deputy Director personally took charge
program, they have involved failure to follow procedures or
                      of the implementation of the Sequoyah CAQR program to ensure
failure to take adequate corrective action.
                      that implementation problems would be resolved. The CAOR
Key positions in the QA department were identified and
                                                                                        . _ _ _ _ - _ _ _
authorities and responsibilities were well defined.
The staff
expertise level was considered excellent.
Trcining contributed
to an adequate understanding of the QA prcgram.
The licensee continued the implementation of the CAQR program
which was established during the basis pericd.
Early in the
'
assessment period CAQR reviews indicated weaknesses in opera-
bility and significance determinations, reviewer and management
training, timeliness, documentation, and auditability of re-
cores. The Sequoyah Site Deputy Director personally took charge
of the implementation of the Sequoyah CAQR program to ensure
that implementation problems would be resolved.
The CAOR
. _ _
_ _ - _ _ _


                                                                            -             ___ ._ _ _ - _ _ - _ _ - _ _ -
-
          '
___ ._ _ _ - _ _ - _ _ - _ _ -
L   .-                                                                                                 .
'
        -
L
p      .
.-
  .
.
    >
p
                                                        49
-
.
49
>
.
1
1
                process required an encrmous amount of dedicated upper nanage-
process required an encrmous amount of dedicated upper nanage-
                ment effort to ensure that it contir:ued to function adequately.
ment effort to ensure that it contir:ued to function adequately.
              .One   major reason that the dedicated management attention was                                           i
.One
major reason that the dedicated management attention was
i
necessary was that a large number of issues were identified at
,
,
                necessary was that a large number of issues were identified at
!
!              Sequoyah, and at other TVA plants which had implications on
Sequoyah, and at other TVA plants which had implications on
                Sequoyah, that required resolution through the corrective action
Sequoyah, that required resolution through the corrective action
                program, resulting in a significant CAQR backlog. A second
program, resulting in a significant CAQR backlog.
                reason was that time-sensitive equipment operabilty determina-
A second
                tions en engineering issues required determinations prior to the
reason was that time-sensitive equipment operabilty determina-
                completion of the CAQR technical evaluations resulting in the
tions en engineering issues required determinations prior to the
                required use of large amounts of predecisional information. The                                           i
completion of the CAQR technical evaluations resulting in the
                corrective action process was determined to be adequate to allow
required use of large amounts of predecisional information. The
                the restart of both units. To this end an order, which dealt
i
                with a management breakdown in controls fcr safety concerns
corrective action process was determined to be adequate to allow
                having generic implications to other TVA sites, was considered
the restart of both units.
                adequately resolved for Sequoyah.
To this end an order, which dealt
                In order to reduce the amount of dedicated upper nanagement
with a management breakdown in controls fcr safety concerns
                effort necessary to make the CAQR system work, the licensee
having generic implications to other TVA sites, was considered
                developed a change to the CAQR process and implemented it in
adequately resolved for Sequoyah.
                September 1988, immediately prior to the restart of Unit 1. The
In order to reduce the amount of dedicated upper nanagement
                change provided several administrative control programs to act
effort necessary to make the CAQR system work, the licensee
                ds Corrective action screening processes. Those issues that did
developed a change to the CAQR process and implemented it in
                not meet the acceptance criteria for being a CAQR stayed in the
September 1988, immediately prior to the restart of Unit 1.
                administrative control programs for resolution. A Quality
The
                Verification Inspection (QVI) conducted near the end o' the
change provided several administrative control programs to act
            -
ds Corrective action screening processes. Those issues that did
                assessment period fcund that the changes were adequately
not meet the acceptance criteria for being a CAQR stayed in the
                implemented and strongly supported by ser.ior line n;anagement.
administrative control programs for resolution.
                The char.ges appeared to have the desired effcct of forcing
A Quality
                insignificant and less significant issues down to the proper
Verification Inspection (QVI) conducted near the end o' the
                level for resolution, while keeping safety significant items at
-
                the senior management level.
assessment period fcund that the changes were adequately
                The QVI reviewed for quality and quality verification in the
implemented and strongly supported by ser.ior line n;anagement.
                areas of plant operations, surveillance, maintenance, corrective
The char.ges appeared to have the desired effcct of forcing
                actions,* modifications, and implementation of commitments made
insignificant and less significant issues down to the proper
                to the NRC. The QVI concluded that site line management was
level for resolution, while keeping safety significant items at
                strongly dedicated to quality and was convincing workers that
the senior management level.
                quality work was what was expected. One exception to this
The QVI reviewed for quality and quality verification in the
                attitude was in the radwaste processing area as revealed by a
areas of plant operations, surveillance, maintenance, corrective
                resin transfer event that occurred at the end of the assessment
actions,* modifications, and implementation of commitments made
                period. This event indicated that management attention had been
to the NRC.
                lacking in the radwaste processing area and that overall site
The QVI concluded that site line management was
                procedure upgrades had not had an effect on upgrading quality in
strongly dedicated to quality and was convincing workers that
                this area.
quality work was what was expected.
                The function c' the quality monitoring organization was to
One exception to this
                assist site management in meeting quality objectives by
attitude was in the radwaste processing area as revealed by a
                identifying ccr.ditions adverse to quality on a real-time basis
resin transfer event that occurred at the end of the assessment
                before they impacted on nuclear safety, reliability, or
period. This event indicated that management attention had been
                                      _ _ _ . _ _ _ _ _   _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ - _ _ _ _ _ _ _ _ _ _ -
lacking in the radwaste processing area and that overall site
procedure upgrades had not had an effect on upgrading quality in
this area.
The function c' the quality monitoring organization was to
assist site management in meeting quality objectives by
identifying ccr.ditions adverse to quality on a real-time basis
before they impacted on nuclear safety, reliability, or
_ _ _ . _ _ _ _ _
_ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ - _ _ _ _ _ _ _ _ _ _ -


                                                                                                  _
_
                                                                                                      _ _ _ _ _ -__
_ _ _ _ _ -__
                                '-
'-
  ,  : .;
: .;
  7
,
      -
7
                                                                  50
50
    ,
-
                                          component' operability.   The quality monitoring organization was
,
                                          observed to be a well qualified and adequately staffed
component' operability.
                                          organization which was adequately performing its function.
The quality monitoring organization was
                                          The use of interfaces between groups, by the organization as a
observed to be a well qualified and adequately staffed
                                          whole, to verify and accept quality when deliverables were
organization which was adequately performing its function.
                                          trar,sferred was not emphasized as a quality verification tool.
The use of interfaces between groups, by the organization as a
                                          For example, the maintenance department was using an interface
whole, to verify and accept quality when deliverables were
                                          organization between the shops and QA to ensure that completed
trar,sferred was not emphasized as a quality verification tool.
                                          surveillance tests represented quality work prior to their
For example, the maintenance department was using an interface
                                          transfer to QA for review, however some of the problems that
organization between the shops and QA to ensure that completed
                                          were being identified for correction had resulted because
surveillance tests represented quality work prior to their
                                          procedure changes had not been adequately communicated to the
transfer to QA for review, however some of the problems that
                                          shop organization responsible for perfchaine them. An interface
were being identified for correction had resulted because
                                          problem was also identified between engineering and the plant in
procedure changes had not been adequately communicated to the
                                          relation to vendor manuals having conflicting data and resulted
shop organization responsible for perfchaine them. An interface
                                          from a lack of communication between the two organizations.                   ;
problem was also identified between engineering and the plant in
                                          Although interface problems between engineering and the plant
relation to vendor manuals having conflicting data and resulted
                                          were identified by the NRC staff during the basis period, inter-
from a lack of communication between the two organizations.
                                          faces were-not actively used by site or corporate mar,agement for
;
                                          the purpose of quality verification.
Although interface problems between engineering and the plant
                                          The licensee identified that the percentage of Boron-10 isotope
were identified by the NRC staff during the basis period, inter-
                                          in the boron being added to the reactor coolant was outside of
faces were-not actively used by site or corporate mar,agement for
                                          the established procurer:ent and design specifications. Although
the purpose of quality verification.
                                          this and related nonconforming ccnditions were identified by
The licensee identified that the percentage of Boron-10 isotope
                                          licensee personnel on at least three distinct occasiens, the
in the boron being added to the reactor coolant was outside of
                                          established corrective action process ecs not implemented in a
the established procurer:ent and design specifications.
                                          timely manner and was only initiated after the issue was raised
Although
                                          by the NRC. Once identified by the licensee, corrective actient
this and related nonconforming ccnditions were identified by
                                          were adequate.
licensee personnel on at least three distinct occasiens, the
                                          The licensee's 10 CFR 50.59 program was reviewed and in most
established corrective action process ecs not implemented in a
                                          cases found to comply with minimum regulatory requirements,
timely manner and was only initiated after the issue was raised
                                          however weaknesses were identified. The first weakness was
by the NRC. Once identified by the licensee, corrective actient
                                          identified as a violation and related to non-conservative
were adequate.
                                          translation of regulatory requirements into procedures; the
The licensee's 10 CFR 50.59 program was reviewed and in most
                                          second weakness was related to the lack of qualification
cases found to comply with minimum regulatory requirements,
                                          requirements for the performance of screening reviews; the third
however weaknesses were identified.
                                          weakness was related to a lack of definition for when
The first weakness was
                                          interdisciplinary reviews were required, and the fourth weakness
identified as a violation and related to non-conservative
                                          was related to coordination of the reviews between groups.
translation of regulatory requirements into procedures; the
                                          These weaknesses indicated minimal management involvement in
second weakness was related to the lack of qualification
                                          assuring the quality of this function. In addition, a failure
requirements for the performance of screening reviews; the third
                                          of the 10 CFR 50.59 process was identified in relation to the
weakness was related to a lack of definition for when
interdisciplinary reviews were required, and the fourth weakness
was related to coordination of the reviews between groups.
These weaknesses indicated minimal management involvement in
assuring the quality of this function.
In addition, a failure
of the 10 CFR 50.59 process was identified in relation to the
excessive post trip cooldown effect on shutdown margin which was
,
,
                                          excessive post trip cooldown effect on shutdown margin which was
identified early in the assessment period and issued after the
                                          identified early in the assessment period and issued after the
end of the assessment period as a Severity 1.evel III violation.
                                          end of the assessment period as a Severity 1.evel III violation.
1
1
A reorganization of the Plant Operations Review Staff (PORS),
'
'
                                          A reorganization of the Plant Operations Review Staff (PORS),
i
i
                                          which is responsible for reporting and investigating plant
which is responsible for reporting and investigating plant
'
'
                                          events, occurred at the beginning of the assessment period.               NRC
events, occurred at the beginning of the assessment period.
          - _ _ _ _ _ - - _ _ _ _ _ - _-             _
NRC
- _ _ _ _ _ - - _ _ _ _ _ - _-
_


              ___       _
___
l;             ,
_
                      ..
l;
                  .
..
              ..                                   51
,
                            concerns about inadeouate root cause analysis for- plant events
.
                            were addressed by prcviding training for the PCRS staff. Root
51
                            cause determinations and licensee corrective actions improved
..
                            throughout the SALP period and have becore more reliable and
concerns about inadeouate root cause analysis for- plant events
                            technically correct near the end of the period. One failure of
were addressed by prcviding training for the PCRS staff.
Root
cause determinations and licensee corrective actions improved
throughout the SALP period and have becore more reliable and
technically correct near the end of the period. One failure of
the root cause reviews was in the area of excessive post trip
'
cooldowns and the resulting effect on end-of-life shutdown
margin which was issued after the end of the assessment period
;
as a Severity Level 111 violation.
The objective for ISEG and the other safety review committees to
identify underlyinc problems before they become issues was
recognized by TVA management.
The safety comnrittee reorganiza-
tions which occurred near the end of the basis perioc began to
have an effect in accomplishing that objective during the
assessment period.
PORC was more aggressive and technically
involved in the resolution of issues affecting the safe
operation of the units.
PORC improvements were due to
consistency in perscnnel staffing, strong leadership from the
new plant manager, and use of the Plant Operations Review Staff
(PORS) as a part-time support group for PORC.
FORS employed
specialized training end skills to perform root cause
evaluations and determine corrective action plans associated
with plant events, which were then submitted a:. completed
projects te PORC.
The use of the P0RS to perform investigative
data gathering and initial evaluat. ions has allowed PORC to be
more deeply involved in day-to-day plant eversight.
The NSRB
'
'
                            the root cause reviews was in the area of excessive post trip
has continued to chcw a low profile with respect to crisite
                            cooldowns and the resulting effect on end-of-life shutdown
ectivities functioning principally in the areas of LER
;                          margin which was issued after the end of the assessment period
evaluation, TS change approval and cther area:: that allow fcr
                            as a Severity Level 111 violation.
offsite review.
                            The objective for ISEG and the other safety review committees to
The ISEG was reorganized as a result of a
                            identify underlyinc problems before they become issues was
TS change and became more aware of industry issues, showed a
                            recognized by TVA management. The safety comnrittee reorganiza-
greater presence in the plant, and by the end of the assessment
                            tions which occurred near the end of the basis perioc began to
period, was becoming an effective auditor of piant activities.
                            have an effect in accomplishing that objective during the
Near the end of the period, ISEG and the other safety committees
                            assessment period.    PORC was more aggressive and technically
were working together better in understanding what each of their
                            involved in the resolution of issues affecting the safe
roles should be in accomplishing the overall objective.
                            operation of the units.      PORC improvements were due to
j
                            consistency in perscnnel staffing, strong leadership from the
l
                            new plant manager, and use of the Plant Operations Review Staff
A broad spectrum of safety issues was identified by TVA
                            (PORS) as a part-time support group for PORC. FORS employed
employees in the ECTG program which reflected a previous lack of
                            specialized training end skills to perform root cause
management involvement with quality.
                            evaluations and determine corrective action plans associated
The NRC staff review of
                            with plant events, which were then submitted a:. completed
the Sequoyah ECTG investigations, corrective actions, and
                            projects te PORC. The use of the P0RS to perform investigative
planned programmatic improvements concluded that the evaluations
                            data gathering and initial evaluat. ions has allowed PORC to be
were generally adequate and well documented.
                    '
I
                            more deeply involved in day-to-day plant eversight. The NSRB
i
                            has continued to chcw a low profile with respect to crisite
I
                            ectivities functioning principally in the areas of LER
The Employee Concerns Program (ECP) continued to be implemented
                            evaluation, TS change approval and cther area:: that allow fcr
in an impressive and professional rcnner.
                            offsite review. The ISEG was reorganized as a result of a
Several audits cf ECP
                            TS change and became more aware of industry issues, showed a
open files ar.c' concerns were completed with no significant
                            greater presence in the plant, and by the end of the assessment
1
                            period, was becoming an effective auditor of piant activities.
l
                            Near the end of the period, ISEG and the other safety committees
findings or wealnesses.
                            were working together better in understanding what each of their
Restart determinations performed on
                            roles should be in accomplishing the overall objective.           j
open files and concerns were accurate and conservative.
                                                                                              l
Followup on issues which were both NRC issues and ECP issues
                            A broad spectrum of safety issues was identified by TVA
]
                            employees in the ECTG program which reflected a previous lack of
                            management involvement with quality.     The NRC staff review of
                            the Sequoyah ECTG investigations, corrective actions, and
                            planned programmatic improvements concluded that the evaluations
                            were generally adequate and well documented.                     I
                                                                                              i
                                                                                              I
                            The Employee Concerns Program (ECP) continued to be implemented
                            in an impressive and professional rcnner. Several audits cf ECP
                            open files ar.c' concerns were completed with no significant     1
                                                                                              l
                            findings or wealnesses. Restart determinations performed on
                            open files and concerns were accurate and conservative.
                            Followup on issues which were both NRC issues and ECP issues
                                                                                              ]
_ _ _ _ _ . _
_ _ _ _ _ . _


                                                                          _ _ _ _ _ _ _
_ _ _ _ _ _ _
                                                                                        ___-
___-
      -
:
:
f   .
-
  .                               52
f
                      ,
.
          resulted in parallel, conservative conclusions.         The ECP
52
          encouraged the return of issues to line managenent for
.
          resolution ar.d in dolng so, has strengthened line inanagement
,
          responsiveness to issues identified by non-canagement employees.
resulted in parallel, conservative conclusions.
          There was a tremendous amount of activity in the licensing area.
The ECP
          Supplemental information regarding licensing ectivity is
encouraged the return of issues to line managenent for
          provided in Section F, under Supporting Data and Summmaries.
resolution ar.d in dolng so, has strengthened line inanagement
          Generally, the large majority of the work done by TVA on
responsiveness to issues identified by non-canagement employees.
          licensing issues was good and showed evidence cf prior plenning
There was a tremendous amount of activity in the licensing area.
          by management.   Hcwever, TVA had a tendency to be optimistic in
Supplemental information regarding licensing ectivity is
provided in Section F, under Supporting Data and Summmaries.
Generally, the large majority of the work done by TVA on
licensing issues was good and showed evidence cf prior plenning
by management.
Hcwever, TVA had a tendency to be optimistic in
'
establishing submittal dates which has resulted in frequent
i
requests for extensions.
Ir. addition, two examples, TSCR 87-47,
Control Poom Emerger.cy Ventilation System, and ISCR CC-21, River
Water Level and Temperature, were noted where TVA knew that a TS
l
change would be needed and the submittals were not made on a
timely basis,
Submittals by TVA generally shcwed an understanding of the
i
i
          establishing submittal dates which has resulted in frequent
          requests for extensions. Ir. addition, two examples, TSCR 87-47,
'
'
          Control Poom Emerger.cy Ventilation System, and ISCR CC-21, River
technical issues beinD discussed.
          Water Level and Temperature, were noted where TVA knew that a TS
The approach to the technical
l
l
          change would be needed and the submittals were not made on a
issues exhibited conservatism and were viable, thorough, and
          timely basis,
j
i
generally sound as demonstrated in their quick response to a
          Submittals by TVA generally shcwed an understanding of the
          technical issues beinD discussed. The approach to the technical
'
l
l
          issues exhibited conservatism and were viable, thorough, and
primary to secondary leak that developed in a Unit 2 steam
j          generally sound as demonstrated in their quick response to a
generator during start-up, in their response to hCC Eulletin
l
88-02, " Rapidly Propagating Tatigue Cracks in Steam Gercrator
          primary to secondary leak that developed in a Unit 2 steam
Tubes", and in their sube ttals requesting relie' from ASNE code
          generator during start-up, in their response to hCC Eulletin
d
          88-02, " Rapidly Propagating Tatigue Cracks in Steam Gercrator
Section XI, inservice Inspection and Operating Plant Cece.
          Tubes", and in their sube dttals requesting relie' from ASNE code
In
          Section XI, inservice Inspection and Operating Plant Cece. In
additicn, TWs proposal tc revise ira;trument accuracy
          additicn, TWs proposal tc revise ira;trument accuracy
calculations for the PCP undervoitage reactor protection channel
          calculations for the PCP undervoitage reactor protection channel
in TSCR 87-18, RCP uncervoltege reactcr trip, could Le censidertd
          in TSCR 87-18, RCP uncervoltege reactcr trip, could Le censidertd
illustrative of a rigorous evaluation cf technical problems and
          illustrative of a rigorous evaluation cf technical problems and
a timely update consistent with ir.dustry practice.
          a timely update consistent with ir.dustry practice. This,
This,
          however, was t.ot true for TSCR 88-T0, Upper lieed Injectinn
however, was t.ot true for TSCR 88-T0, Upper lieed Injectinn
          Accumulator Level Switch Setpoint which was submitted without
Accumulator Level Switch Setpoint which was submitted without
          TVA understanding thet its application dia net meet 10 Cfh
TVA understanding thet its application dia net meet 10 Cfh
          50.46(a)(1) and therefore required an exarption.
50.46(a)(1) and therefore required an exarption.
          Conservatism in the licensee's alternate approach tc problems
Conservatism in the licensee's alternate approach tc problems
          was generally exhibited and decisicn making was usually at a
was generally exhibited and decisicn making was usually at a
          level that ensured adequete managerent review. The technical
level that ensured adequete managerent review.
          reviews occasicnbily were lecting in detail and/cr technical
The technical
          basis.     Licensee statements at meetings were not always well
reviews occasicnbily were lecting in detail and/cr technical
          thought cut prior to presentation to the NRC indicating that
basis.
          communication between licensee organizations was not always
Licensee statements at meetings were not always well
          clear.
thought cut prior to presentation to the NRC indicating that
          TVA was generally responsive to NRC initiatives.           NRC
communication between licensee organizations was not always
            expectations regarding the issue of Ste6m Binding of Acxiliary
clear.
            Feedwater (AFW) pumps were met in the area of technical accuracy
TVA was generally responsive to NRC initiatives.
            and were exceeded in the area of scheduling. The overall
NRC
_       -
expectations regarding the issue of Ste6m Binding of Acxiliary
Feedwater (AFW) pumps were met in the area of technical accuracy
and were exceeded in the area of scheduling.
The overall
_
-


        __ _ __. _                                                                       _
__ _ __. _
                                                                                              _ _ . _ _ _ _                     _
_
                                                                                                                                          ,   ._ __     __ _ _ _ ___
_ _ . _ _ _ _
,
_
  ,:              '
,
                                        .
._ __
    ,'
__
t
_ _ _ ___
Y s.                                                                                                               S3
'
                                                                            staffing to support operating activities was adequate with the
,:
>y.                                                                         licensing engineer-being well qualified and adequately trained.
,
                                                                            - The site licensing organization has been successful in improving-                       1
.
h                                                                         . the timeliness and quality of responses to NRC violations.
,'
                                                                                                                                                                      '
t
                                                                            TVA Nuclear Power cor) orate management was usually involved in
Y s.
                                                                            Sequoyah site activit'es in an effective manner. The corporate
S3
                                                                            level was reorganized on-~ July 1,1988, as part of a general
staffing to support operating activities was adequate with the
                                                                              reorganization of TVA itself, and resulted in a reduction in the
>y.
                                                                            number of levels of management between the Senior Vice President-
licensing engineer-being well qualified and adequately trained.
                                                                            Nuclear Power, who is manager of the TVA nuclear power program,
- The site licensing organization has been successful in improving-
                                                                            and the site.                 Also, the manager of the TVA nuclear power
1
                                                                            program, who was a contract employee, was replaced by a perma-
h
                                                                            nent TVA employee. The emphasis of TVA's nuclear power program
. the timeliness and quality of responses to NRC violations.
                                                                              has switched.to operating the Sequoyah units within constrained
TVA Nuclear Power cor) orate management was usually involved in
                                                                            TVA budgets, compared to past budgets, and reduction-in-force
'
                                                                            within TVA's nuclear power program including the site. The
Sequoyah site activit'es in an effective manner.
                                                                              effects of the new emphasis is ur.certain, however, the NRC has
The corporate
                                                                              noted that TVA was reassessing the' dates and scope for commit-
level was reorganized on-~ July 1,1988, as part of a general
                                                                            ments.
reorganization of TVA itself, and resulted in a reduction in the
                                                                              Corporate support for site activities was observed in the areas
number of levels of management between the Senior Vice President-
                                                                              of Operations, Quality Assurance, and outage inanagement.                 The
Nuclear Power, who is manager of the TVA nuclear power program,
                                                                              support in these areas was limited to activities and managers
and the site.
                                                                              necessary . to support the restart of Units 1 and 2 and the
Also, the manager of the TVA nuclear power
                                                                              refueling of Unit 2.                 The support was not global in nature and
program, who was a contract employee, was replaced by a perma-
    .                                                                        consisted mainly of loaned corporate managers and specialists
nent TVA employee.
                                                                              that met specified needs.                 Activities appeared to be well
The emphasis of TVA's nuclear power program
                                                                              supported by corpor~ ate management and the mai. agers supplied by
has switched.to operating the Sequoyah units within constrained
                                                                              corporate management were professional and well suited to the
TVA budgets, compared to past budgets, and reduction-in-force
                                                                              assigned tasks. A site Radiological Assessor position has been
within TVA's nuclear power program including the site.
                                                                              established.                 The position reports to the Manager of
The
                                                                              Radiological Control, a corporate position rather than to the
effects of the new emphasis is ur.certain, however, the NRC has
                                                                              Site Director. The position provides a programmatic cverview of
noted that TVA was reassessing the' dates and scope for commit-
                                                                              the- Sequoyah radiological control program and an independent
ments.
                                                                              reporting path offsite.                 The Site / Corporate interface was
Corporate support for site activities was observed in the areas
                                                                              adequate and programmatic overview of the site was occurring.
of Operations, Quality Assurance, and outage inanagement.
                                                                              For the assessment period, ccrporate mt.negement continued to be
The
                                                                              generally responsive to NRC initiatives. The responses to NRC
support in these areas was limited to activities and managers
                                                                              were generally timely, sound and thorough. /ilthough Unit I was
necessary . to support the restart of Units 1 and 2 and the
                                                                              restarted in November 1988, the restart date was only three
refueling of Unit 2.
                                                                              months later than originally scheduled by TVA, as compared to
The support was not global in nature and
(.                                                                           two years later for Unit 2, which showed evidence of improved
consisted mainly of loaned corporate managers and specialists
L                                                                             planning and assignment of priorities.
.
                                                                              .The significant exceptions to TVA's general responsiveness to
that met specified needs.
                                                                              NRC initiatives and timely submittals in the rating period were
Activities appeared to be well
                                                                              the resolution of the silicone rubber insulated cable testing
supported by corpor~ ate management and the mai. agers supplied by
                                                                              issue and the tardiness of TVA in submitting Revision E of the
corporate management were professional and well suited to the
                                                                              Corporate Nuclear Performance Plan to reflect the July 1,1988
assigned tasks.
                                                                              reorganization.
A site Radiological Assessor position has been
                                                                          .
established.
      I             _ _ _ _ _ _ _ _ _ . _ _ _ . _ _ _ . . . . , _ . . _,
The position
reports
to the Manager of
Radiological Control, a corporate position rather than to the
Site Director. The position provides a programmatic cverview of
the- Sequoyah radiological control program and an independent
reporting path offsite.
The Site / Corporate interface was
adequate and programmatic overview of the site was occurring.
For the assessment period, ccrporate mt.negement continued to be
generally responsive to NRC initiatives.
The responses to NRC
were generally timely, sound and thorough. /ilthough Unit I was
restarted in November 1988, the restart date was only three
months later than originally scheduled by TVA, as compared to
(.
two years later for Unit 2, which showed evidence of improved
L
planning and assignment of priorities.
.The significant exceptions to TVA's general responsiveness to
NRC initiatives and timely submittals in the rating period were
the resolution of the silicone rubber insulated cable testing
issue and the tardiness of TVA in submitting Revision E of the
Corporate Nuclear Performance Plan to reflect the July 1,1988
reorganization.
.
I
_ _ _ _ _ _ _ _ _ . _ _ _ . _ _ _ . . . . , _ . . _,


    - _ _ -                                   _ _ _ _ _ _ _
- _ _ -
                    '
_ _ _ _ _ _ _
  .
'
    9                                                                                         P
.
9
P
54
-
Seven violations were identified:
a.
Severity Level IV violation for failure to follow
procedures for authorization to exceed plant overtime
limits.(327,328/87-70-01)
b.
Severity Level IV violation for failure to follow
procedures for installation and inspection of seal table
bolts. (327, 328/88-09-01)
c.
Severity Level IV violation for failure to take prompt
corrective action for deficiencies in QA record storage.
(327,328/88-09-02)
l
d.
Severity Leve'l IV violation for failure to properly
translate 10 CFR 50.59 requirements into instructions or
procedures.
(327,328/88-43-01)
e..
Severity Level IV violation for failure to take adequate
corrective action for prevention of reactivity changes
while both trains of control room ventilation are
inoperable. (88-27-01)
!
f.
Severity Level IV violation for failure to. take adequate
'
corrective action to preclude repetition of violation
87-S0-01 involving lack of control over plant evolutions,
,
and system and equipment status in the radioactive weste
-
-
                                                                                                54
area.
                                                                      Seven violations were identified:
(88-50-01)
                                                                      a.   Severity Level IV violation for failure to follow
g.
                                                                            procedures for authorization to exceed plant overtime
Severity Level IV violation for three examples of failure
                                                                            limits.(327,328/87-70-01)
to promptly identify and initiate adequate corrective
                                                                      b.  Severity Level IV violation for failure to follow
action for Boron-10 procurement problems.
                                                                            procedures for installation and inspection of seal table
(88-60-01)
                                                                            bolts. (327, 328/88-09-01)
l
                                                                      c.  Severity Level IV violation for failure to take prompt
2.
                                                                            corrective action for deficiencies in QA record storage.
Performance Rating
                                                                            (327,328/88-09-02)
' Category: 2
                                                                      d.  Severity Leve'l IV violation for failure to properly      l
3.
                                                                            translate 10 CFR 50.59 requirements into instructions or
Recommendations
                                                                            procedures.  (327,328/88-43-01)
None
                                                                      e..  Severity Level IV violation for failure to take adequate
j
                                                                            corrective action for prevention of reactivity changes
V.
                                                                            while both trains of control room ventilation are
SUPPORTING DATA AND SUMMARIES
                                                                            inoperable. (88-27-01)
l
                                                                                                                                      !
A.
                                                                            Severity Level IV violation for failure to. take adequate
Investigation Review
                                                                                                                                      '
The NRC's Office of Investigations closed fourteen cases which dealt
                                                                      f.
with TVA during the assessrrent period.
                                                                            corrective action to preclude repetition of violation
None of these involved
                                                                            87-S0-01 involving lack of control over plant evolutions, ,
enforcement action pertaining to Sequcyah.
                                                                            and system and equipment status in the radioactive weste  -
l
                                                                            area.   (88-50-01)
1
                                                                      g.  Severity Level IV violation for three examples of failure
-_ _ __ . _ - _ _ _ _ _ _ _ _ _ _
                                                                            to promptly identify and initiate adequate corrective
                                                                            action for Boron-10 procurement problems.   (88-60-01)   l
                                                                2.   Performance Rating
                                                                    ' Category: 2
                                                                3.   Recommendations
                                                                      None                                                           j
                            V.                             SUPPORTING DATA AND SUMMARIES
                                                                                                                                      l
                                                            A.   Investigation Review
                                                                The NRC's Office of Investigations closed fourteen cases which dealt
                                                                with TVA during the assessrrent period. None of these involved
                                                                enforcement action pertaining to Sequcyah.
                                                                                                                                      l
                                                                                                                                      1
            -_ _ __ . _ - _ _ _ _ _ _ _ _ _ _


!.                                                                                 .                                                    1
!.
                '
1
  l       .
.
            .
l
'
.
L
L
        .                                                                                 55
.
!                                             B.. Escalated Enforcement Action
55
                                                  1.             Civil Penalties
.
                                                                                                                                        4
!
                                                                  Severity Level III violation issued on July 3,1988, concerning
B..
                                                                  failure to ccmply with TS when both centrifugal charging pumps
Escalated Enforcement Action
                                                                  were inoperable and failure to report this condition pursuant to
1.
                                                                  10 CFR 50.72. ($50,000 CP)
Civil Penalties
4
Severity Level III violation issued on July 3,1988, concerning
failure to ccmply with TS when both centrifugal charging pumps
were inoperable and failure to report this condition pursuant to
10 CFR 50.72. ($50,000 CP)
,.
,.
                                                  2.             Discretionary Enforcement for Shutdown Plants
2.
                                                                  Failure to meet the 10 CFP 50.59 requirements for a 1984
Discretionary Enforcement for Shutdown Plants
                                                                  auxiliary feedwater pump modification.       No Notice of Violation
Failure to meet the 10 CFP 50.59 requirements for a 1984
                                                                  or Civil Penalty was issued as discussed in a letter dated
auxiliary feedwater pump modification.
                                                                  May 9, 1988.
No Notice of Violation
                                              C.   Licensee Conferences Held During Appraisal Period
or Civil Penalty was issued as discussed in a letter dated
                                                  During the appraisal period, meetings were held with the licensee to
May 9, 1988.
                                                  discuss various issues, as follows:
C.
                                                  1. Management Meetings
Licensee Conferences Held During Appraisal Period
                                                                  Date                                   Purpose
During the appraisal period, meetings were held with the licensee to
                                                                  February 11, 1988   Meeting to discuss load sequencing of
discuss various issues, as follows:
                                                                                        plant diesel generators.
1. Management Meetings
                                                                  March 09, 1988       Meeting to discuss technical issues related
Date
                                                                                        to 10 CFR 50 Appendix R.
Purpose
                                                                  April 14, 1988       Meeting to discuss differences between
February 11, 1988
                                                                                        Sequoyah, Units 1 and 2 in the Sequoyah
Meeting to discuss load sequencing of
                                                                                        Nuclear Performance Plcn.
plant diesel generators.
                                                                  April 29, 1988       Meeting to discuss (1) the Unit 2 steam
March 09, 1988
                                                                                        generator tube leakage and (2) loop seals     '
Meeting to discuss technical issues related
                                                                                                                                      .
to 10 CFR 50 Appendix R.
                                                                                        for the pressurizer safety valves.
April 14, 1988
                                                                  June 13, 1988         l'eeting to discuss the restart of Unit 2 in
Meeting to discuss differences between
                                                                                        light of the five scrams from power in
Sequoyah, Units 1 and 2 in the Sequoyah
                                                                                        May 1988.
Nuclear Performance Plcn.
                                                                  June 22, 1988         Meeting to discuss the TVA commitments for
April 29, 1988
                                                                                        Unit ?.
Meeting to discuss (1) the Unit 2 steam
                                                                  July 21, 1988         Meeting to discuss Phase II of the Design
generator tube leakage and (2) loop seals
                                                                                        Baseline and Verification Program fcr
.
                                                                                        Sequoyah.
'
                                                                  September 8, 1988     Meeting to discuss changes to the TVA
for the pressurizer safety valves.
                                                                                        Conditions Adverse to Quality Program at
June 13, 1988
                                                -
l'eeting to discuss the restart of Unit 2 in
                                                                                        Sequoyah.
light of the five scrams from power in
    _ _     _ - _ - _ - _ _ _ _ _ _ _ _ _ _         _ _ _ _ _ -         - _ _ _ .
May 1988.
June 22, 1988
Meeting to discuss the TVA commitments for
Unit ?.
July 21, 1988
Meeting to discuss Phase II of the Design
Baseline and Verification Program fcr
Sequoyah.
September 8, 1988
Meeting to discuss changes to the TVA
Conditions Adverse to Quality Program at
-
Sequoyah.
_ _
_ - _ - _ - _ _ _ _ _ _ _ _ _ _
_ _ _ _ _ -
- _ _ _ .


                              - _-_.                 . _ _ -
- _-_.
                                                  '
. _ _ -
                  .
'
                    4
.
              *
4
                                                                                          56
56
                                                                  September 13, 1988 Meeting to discuss TVA's preparation for
*
                                                                                      Unit I restart and the post-trip cooldown
September 13, 1988 Meeting to discuss TVA's preparation for
                                                                                      shutdown margin issue.
Unit I restart and the post-trip cooldown
                                                                  September 15, 1988 Meeting on TVA's Microbiological 1y
shutdown margin issue.
                                                                                      Induced Corrosion Program at Sequoyah.
September 15, 1988 Meeting on TVA's Microbiological 1y
                                                                  October 24, 1988     Meeting on the status of TVA's commitments
Induced Corrosion Program at Sequoyah.
                                                                                      to NRC on Sequoyah.
October 24, 1988
                                                                  November 28, 1988   Meeting on the Essential Raw Cooling Water
Meeting on the status of TVA's commitments
to NRC on Sequoyah.
November 28, 1988
Meeting on the Essential Raw Cooling Water
pumphouse formulation and roadway access
'.
'.
                                                                                      pumphouse formulation and roadway access
cells.
                                                                                      cells.
2.
                                                              2. Enforcement Conferences
Enforcement Conferences
                                                                  March 17, 1988       Enforcement     Conference   at Sequoyah
March 17, 1988
                                                                                      concerning     centrifugal   charging pump
Enforcement
                                                                                      operability which resulted in EA 88-86.
Conference
                                                                                      (IR 88-20)
at
                                                                  July 28, 1988       Enforcement Conference at Sequoyah
Sequoyah
                                                                                      concerning upper head injection system
concerning
                                                                                      operability. Issued as Severity Level IV.
centrifugal
                                                                                        (IR88-34)
charging
                                                                  December 19, 1988   Enforcement Conference at NRC Headquarters
pump
                                                                                      concerning the affect of excessive cooldewns
operability which resulted in EA 88-86.
                                                                                      following reactor trips on end-of-life
(IR 88-20)
                                                                                      shutdown margin which resulted in EA 88-307.
July 28, 1988
                                                                                        (IR 88-35 & 88-55)
Enforcement Conference at Sequoyah
                                                    D.       Confirmation of Action Letters
concerning upper head injection system
                                                              1.   April 26, 1988             Reinstatement of Hold Points for
operability. Issued as Severity Level IV.
                                                                                              Unit 2 Restart from Steam Generator
(IR88-34)
                                                                                              Outage
December 19, 1988
                                                              2.   June 16, 1988             Confirmation of Release from Unit 2
Enforcement Conference at NRC Headquarters
                                                                                              Hold Points
concerning the affect of excessive cooldewns
                                                              3.   November 7, 1988           Reinstatement of Unit 1 Mode 2 Hold
following reactor trips on end-of-life
                                                                                              Point
shutdown margin which resulted in EA 88-307.
                                                                                                                                    a
(IR 88-35 & 88-55)
  _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ .
D.
Confirmation of Action Letters
1.
April 26, 1988
Reinstatement of Hold Points for
Unit 2 Restart from Steam Generator
Outage
2.
June 16, 1988
Confirmation of Release from Unit 2
Hold Points
3.
November 7, 1988
Reinstatement of Unit 1 Mode 2 Hold
Point
a
_ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ .


        _ _ _ _                   _
_ _ _ _
                '
_
        .
'
        .
.
  , .                                                                       57
.
                                  E. Review of Licensee Event Reports
, .
                                      During the assessment period, there were a total of 78 LERs analyzed
57
                                      for Units 1 & 2. The distribution of these reports by causes, as
E.
                                      determined by the hRC staff was as follows:
Review of Licensee Event Reports
                                      LER CAUSES                                         UNIT 1 UNIT 2
During the assessment period, there were a total of 78 LERs analyzed
                                      Component failure       ................. 2                 6
for Units 1 & 2.
                                      Design ............................ 2                       1
The distribution of these reports by causes, as
                                      Construction / Installation /.......... 1                   3
determined by the hRC staff was as follows:
                                        Fabrication
LER CAUSES
                                      Inadequate Procedure............... 11                     3
UNIT 1
                                      Test Calibration.................... 7                     3
UNIT 2
                                      0ther............................... 7                     3
Component failure
                                      Personnel
................. 2
                                      - operati ng acti vity. . . . . . . . . . . . . . . . 5     6
6
                                      - maintenance activity..............                 2     4
Design ............................ 2
                                      - test / calibration..................               2     6
1
                                      - other............................. 3                     1
Construction / Installation /.......... 1
                                      Total                                               42   36
3
                                  F. Licensing Activities
Fabrication
                                      The assessment of licensing activities was based, in part, upon
Inadequate Procedure...............
                                      licensing actions successfully completed duri,ng this period. These
11
      -                              include the following:
3
                                      1.   Discretionary Enforcement /ilaiver of Compliance
Test Calibration....................
                                            January 30, 1989                   Emergency Diesel Generator Surveillance
7
                                                                                Testing
3
                                      2.   Reliefs Granted
0ther...............................
                                            February 8,1988                     American Society of flechanical
7
                                                                                Engineers (ASME) Code Case N-411
3
                                            May 11, 1988                       ASME Code Section XI Relief for the
Personnel
                                                                                Microbiologically Induced Corrosion
- operati ng acti vity. . . . . . . . . . . . . . . . 5
                                                                                (MIC) Program
6
                                            August 18, 1988                     Hydrogen Analyzer Sampling Valves,
- maintenance activity..............
                                                                                ASf1E Code.Section XI Relief
2
                                            September 15, 1988                   ERCW Valves on CSS Heat Exchangers,
4
                                                                                ASME Code Section XI Relief
- test / calibration..................
                                            September 15, 1988                   Generic Relief on Use of Ultrasonic
2
                                                                                Monitoring of Pump Flow
6
                                            November 4, 1988                     Temporary Deviation from Appendix R to
-
                                                                                to 10 CFR 50, Section III.G.
other.............................
.     .
3
                  _ _ _ - _ _ _ _
1
Total
42
36
F.
Licensing Activities
The assessment of licensing activities was based, in part, upon
licensing actions successfully completed duri,ng this period.
These
include the following:
-
1.
Discretionary Enforcement /ilaiver of Compliance
January 30, 1989
Emergency Diesel Generator Surveillance
Testing
2.
Reliefs Granted
February 8,1988
American Society of flechanical
Engineers (ASME) Code Case N-411
May 11, 1988
ASME Code Section XI Relief for the
Microbiologically Induced Corrosion
(MIC) Program
August 18, 1988
Hydrogen Analyzer Sampling Valves,
ASf1E Code.Section XI Relief
September 15, 1988
ERCW Valves on CSS Heat Exchangers,
ASME Code Section XI Relief
September 15, 1988
Generic Relief on Use of Ultrasonic
Monitoring of Pump Flow
November 4, 1988
Temporary Deviation from Appendix R to
to 10 CFR 50, Section III.G.
.
.
_ _ _ - _ _ _ _


                                                                                                        -___--_ -_ - __ -
.
                                                                                                  .
-___--_ -_ - __ -
                                                            _
_
,    c.-
c.-
-.
,
-                                                                               58
-.
                                                    3.     Exemptions
58
                                                          July 14,_1988             Schedular Exemption to Appendix J,
-
                                                                                    Type B and C Testing
3.
                                                          September 22, 1988       Exemption to Appendix J. Type C
Exemptions
                                                                                    -Testing for C/RHR Spray System Check
July 14,_1988
                                                                                    Valves
Schedular Exemption to Appendix J,
                                                          October 26, 1988         Temporary Exemption to Appendix K ECCS
Type B and C Testing
                                                                                    Calculations to May 31, 1989
September 22, 1988
                                                          January 26, 1989         Exemption to 10 CFR 50.46(a)(1),
Exemption to Appendix J. Type C
                                                                                    Approved ECCS Analysis for Operating-
-Testing for C/RHR Spray System Check
                                                                                    Cycle 4
Valves
                                                    4.   Orders
October 26, 1988
                                                          March 31, 1988           Modification of Order 85-49 stating
Temporary Exemption to Appendix K ECCS
                                                                                    that Sequoyah had satisfied the
Calculations to May 31, 1989
                                                                                    requirements of the Order.
January 26, 1989
                                                      5.   Emergency or Exioent Technical Specification (TS) Amendments,
Exemption to 10 CFR 50.46(a)(1),
                                                          June 30, 1988             Exigent TS /cendment on Ct rporate -
Approved ECCS Analysis for Operating-
                -
Cycle 4
                                                                                    Reorganization
4.
                                                          January 3'0, 1989         Emergency TS Amendment on Diesel
Orders
                                                                                    Generator Surveillance Testing
March 31, 1988
                                                      6.   Malti-Plant Actions (MPA) Resolved
Modification of Order 85-49 stating
                                                                Date                     MPA Description
that Sequoyah had satisfied the
                                                          fiarch:21, 1988           F-05, Procedures Generation Package
requirements of the Order.
                                                          May 5, 1988               A-21, Pressurized Thermal Shock
5.
                                                          May 18, 1988             B-60, Environmental Qualification
Emergency or Exioent Technical Specification (TS) Amendments,
                                                                                      for Unit 2
June 30, 1988
                                                          July 20, 1988             B-98, Bulletin 85-01, Steam Binding of
Exigent TS /cendment on Ct rporate -
                                                                                      AFW Pumps
-
                                                          September 9, 1988         B-101, Boric Acid Corrosion of Carbon
Reorganization
            *                                                                        Steel RCS Components
January 3'0, 1989
                                                            November 28, 1988       B-81, GL 83-28, Items 4.2.1/4.2.2
Emergency TS Amendment on Diesel
                                                            February 3, 1989         B-60, Environmental Qualification for
Generator Surveillance Testing
                                                                                      Unit 1                               _
6.
          .
Malti-Plant Actions (MPA) Resolved
' '' -         _ _ _ _ _ . _ _ _ _ _ _ _ _ _ _ _ . _ _ _ _
Date
MPA Description
fiarch:21, 1988
F-05, Procedures Generation Package
May 5, 1988
A-21, Pressurized Thermal Shock
May 18, 1988
B-60, Environmental Qualification
for Unit 2
July 20, 1988
B-98, Bulletin 85-01, Steam Binding of
AFW Pumps
September 9, 1988
B-101, Boric Acid Corrosion of Carbon
Steel RCS Components
*
November 28, 1988
B-81, GL 83-28, Items 4.2.1/4.2.2
February 3, 1989
B-60, Environmental Qualification for
Unit 1
_
.
' '' -
_ _ _ _ _ . _ _ _ _ _ _ _ _ _ _ _ . _ _ _ _


                                                                                                            . _ _ _ _ _ _ - . ._ ______
. _ _ _ _ _ _ - . ._ ______
'
'
                              ..
..
                            ,
,
                            *
*
l
l
                                                                  59
59
                                    7. Significant Plant-Specific Issues Resolved
7.
                                              Date                             Description
Significant Plant-Specific Issues Resolved
                                        February 23, 1988             Sequoyah Pipe Support Criteria
Date
                                        February 23, 1988             Unit 2 Extended Heatup Prior to Restart
Description
                                        March 11, 1988               Unit 2 Restart Employee Concern Element
February 23, 1988
                                                                      Reports
Sequoyah Pipe Support Criteria
                                        March 14, 1988               Revised Sequoyah IST Program
February 23, 1988
                                        March 21, 1988               Hydrogen Analyzer Operability
Unit 2 Extended Heatup Prior to Restart
                                        May 18, 1988                 NUREG-1232, Volume 2, Review of
March 11, 1988
                                                                      Sequoyah Nuclear Performance Plan for
Unit 2 Restart Employee Concern Element
                                                                      Unit 2 Restart
Reports
                                        May 25, 1988                 Silicone Rubber Insulated Cable Inside
March 14, 1988
                                                                                                                                          *
Revised Sequoyah IST Program
                                                                      Containment
March 21, 1988
                                        June 23, 1988                 Bulletin 86-02, Static-0-Ring Switches
Hydrogen Analyzer Operability
                                        Jul.y 6, 1988                 GL 87-06, Periodic Verification of PIV
May 18, 1988
                                                                      Leak Tight Integrity
NUREG-1232, Volume 2, Review of
                                        August 3, 1988               10 CFR 2.206 Petition on Emergercy
Sequoyah Nuclear Performance Plan for
                                                                      Diesel Generators
Unit 2 Restart
                                        September 22, 1988           JC0 for Operation with C/RHR Spray
May 25, 1988
                                              _
Silicone Rubber Insulated Cable Inside
                                                                      System Check Valves without
Containment
                                                                      Appendix J, Type C Testing
*
                                        November 4, 1988             Unit 1 Restart and Both Units
June 23, 1988
                                                                      Non-Restart Employee Concern Element
Bulletin 86-02, Static-0-Ring Switches
                                                                      Reports
Jul.y 6, 1988
                                        December 5, 1988             GL 87-12, Loss of RHR with RCS
GL 87-06, Periodic Verification of PIV
                                                                      Partially Filled
Leak Tight Integrity
                                        February 3,1989               NUREG-1232, Volume 2, Supplement i
August 3, 1988
                                                                      Review of Sequovah Nuclear
10 CFR 2.206 Petition on Emergercy
                                                                      Performance P'       for Unit 1 Restart
Diesel Generators
                                                                                                        .
September 22, 1988
                                                              .
JC0 for Operation with C/RHR Spray
                                                                                                                  d
System Check Valves without
. _ _ _ _ _ _ _ _ _ _ _ _ _       __   __         __ _   _   __       _ _ _       _
_
                                                                                          ______________________________________________;
Appendix J, Type C Testing
November 4, 1988
Unit 1 Restart and Both Units
Non-Restart Employee Concern Element
Reports
December 5, 1988
GL 87-12, Loss of RHR with RCS
Partially Filled
February 3,1989
NUREG-1232, Volume 2, Supplement i
Review of Sequovah Nuclear
Performance P'
for Unit 1 Restart
.
.
d
. _ _ _ _ _ _ _ _ _ _ _ _ _
__
__
__
_
_
__
_ _ _
_
______________________________________________;


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                                                                                                              m et oe        r
                                                                                                                                  on
-                  n    R    id                            ti    ht        ih        hn      en be                        Mor
                    o          li
                                        no    Lr        t    as Cs            LC        S e Ro          al      a    nr          Co
                                                      a s      cy                                                W                      f
                  C    lom be is        oi                              i
                                                                                              m    i  T p              oi
                                      it        si      i i h        en          er eu          Pt          m        iD      ic r
                    r re        aR      ta      sl        n  fP      vi        te        tr  Wa    dI        r    t        moc
                    e tt        r      il
                                                ai      i    i(    l
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                    w ns er do                    px      m  d      ed        l a        ms  At      ed      v dm        i      g
                    o oy po ds                  yu d          oL      wA        eW en Dc mn i du                                eRo
                  L CS        OF      Ai      BA A MO              T(          D(      Ri    TA    Aa R            AP      SSL
            R '
            E    7      7    3      5        3        1          242        3              0      57      1      236    71
              B    3      4    0        1        3        0          1 41        2              1      00      2      443    03
              M      -    -    -        -        -        - R        -    -  -                -      - -    -      - - -    - -
            U    7      7    7        7        7        7  E      778        7        9    8      88      8      777    77
              N    8      8    8        8        8        8  G      888        8        7    8      88      8      888    88
                                                              S
              S S S            S        S        S        S          SSS        S        S    S      SS      S      SSS    SS
              T  T      T    T        T        T        T          TTT        T        T    T      TT      T      TTT    TT
              D
              E
              U    8      8    8      8        8        8    8      8          8          8    8      8      8      8        8
              S    8      8    8      8        8        8    8      8          8          8    8      8      8      8        8
              S / /            /        /        /            /      /          /        /    /      /        / /            /
              I  1      7    4        6        8        4,  7      0          6        3      5      5        5 6            1
                  1      1    0      1        1        2    2      3          0          1    /      1        1      1      /
              E    / /        /        /        /        / /        /          /        /      8      /        / /            9
              T    2 2        4        5        5        5  6      6          7          7    0      8        8    8        0
              A
              D
              2
          O
          NT        9 0        1      2        3        4    5      6            -        7    8      9        0    1        2
              I
                    5 6        6      6        6        6    6      6                    6    6      6        7    7        7
          TN
          NU
          E
          M
          D
          N
          E1
          M
          AT      7      8    9        0      1        2  3      4          5        6    7      8        9    0        1
              I
                  6      6    6      7        7        7  7      7          7        7    7      7        7    8        8
              N
              U
    s
    t
      n
      e
      m                                            -
    d
      n
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      m
    A
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      s
  3  n
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      .
    8
        .


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-


- - -                                                                                                                 _
- - -
          *
_
        .
*
                                                                                                                        l
.
        .
.
      ,                                              63                                                                 i
63
                  G.   Enforcement Activity                                                                               ,
i
                                                                                                                        l
,
                      All violations for the appraisal period were cited against Unit 1                                   I
G.
                      and Unit 2.
Enforcement Activity
                                                                                                                        *
,
                                        NO. OF DEVIATIONS & VIOLATIONS IN SEVERITY LEVEL
l
            FUNCTIONAL
All violations for the appraisal period were cited against Unit 1
              AREA                     DEV       V         IV       III       II                             I
and Unit 2.
            PLANT OPERATIONS           1                   4       1
*
            RADIOLOGICAL CONTROLS                           2
NO. OF DEVIATIONS & VIOLATIONS IN SEVERITY LEVEL
            MAINTENANCE /                         1         16
FUNCTIONAL
              SURYLILLANCE
AREA
            EMERGENCY PREPAREDNESS               1         2
DEV
            SECURITY
V
            ENGINEERING / TECHNICAL                         2
IV
              SUPPORT
III
            SAFETY ASSESSMENT /                             7
II
              QUALITY VERIFICATION
I
            TOTAL                       1         2         33       1
PLANT OPERATIONS
                  H.   Reactor Trips
1
                      A total of seven automatic reactor trips occurred during the
4
                      assessment pericd, five above 15% power and two below 15% power.                       ~
1
                                                                                                                  No
RADIOLOGICAL CONTROLS
                      manual trips were initiated and no trips occurred with the unit
2
                      subcritical. In general, these reactor trips occurred during power
MAINTENANCE /
                      esca11ation activities ano were followed by extended periods cf
1
                      continued operation.   The trips are described in more detail below:
16
                            May 19,1988 - Unit 2 tripped from 73% pcwer due to a steam / feed
SURYLILLANCE
                            flow mismatch coincident with low steam generator level. This
EMERGENCY PREPAREDNESS
                            situation occurred due to maintenance being performed concur-
1
                            rently on two p'ieces of equipment which together could cause a
2
                            reactor trip (one channel of steam generator level indication to
SECURITY
                            replace an unqualified splice and the #3 heater drain tank level
ENGINEERING / TECHNICAL
                            controller which resulted in plant oscillations).
2
                            May 23,1988 - Unit 2 tripped from 70% power due to low flow on
SUPPORT
                            RCS Loop #4. This situation occurred due to a personnel error
SAFETY ASSESSMENT /
                            while performing a surveillance on the Icop #4 flow transmit-
7
                            ters.
QUALITY VERIFICATION
                            June 6,1988 - Unit 2 tripped from 98% power on steam / feed flow
TOTAL
                            mismatch coincident with low level in li4 steam generator. The
1
                            trip occurred while performing a surveillcrce on the feedwater
2
                            regulating valves and resulted because a diode was missing in
33
                            the block circuit.
1
                                                                          _         _ _ _ _ _ _ _ _ _ _ _ _ -       -
H.
Reactor Trips
A total of seven automatic reactor trips occurred during the
assessment pericd, five above 15% power and two below 15% power.
No
manual trips were initiated and no trips occurred with the unit
~
subcritical.
In general, these reactor trips occurred during power
esca11ation activities ano were followed by extended periods cf
continued operation.
The trips are described in more detail below:
May 19,1988 - Unit 2 tripped from 73% pcwer due to a steam / feed
flow mismatch coincident with low steam generator level. This
situation occurred due to maintenance being performed concur-
rently on two p'ieces of equipment which together could cause a
reactor trip (one channel of steam generator level indication to
replace an unqualified splice and the #3 heater drain tank level
controller which resulted in plant oscillations).
May 23,1988 - Unit 2 tripped from 70% power due to low flow on
RCS Loop #4.
This situation occurred due to a personnel error
while performing a surveillance on the Icop #4 flow transmit-
ters.
June 6,1988 - Unit 2 tripped from 98% power on steam / feed flow
mismatch coincident with low level in li4 steam generator. The
trip occurred while performing a surveillcrce on the feedwater
regulating valves and resulted because a diode was missing in
the block circuit.
_
_ _ _ _ _ _ _ _ _ _ _ _ -
-


*:
'
<
<
  '
,
    ,                       *:
e
    e
*
    *                                                             64
64
                                        June 8, 1988 - Unit 2 tripped from 12% power on low-low level in
June 8, 1988 - Unit 2 tripped from 12% power on low-low level in
                                        #2 steam generator due to an operator error when placing the
#2 steam generator due to an operator error when placing the
                                        feed pump controller in the automatic position resulting in
feed pump controller in the automatic position resulting in
                                        steam generator level oscillations.
steam generator level oscillations.
                                        June 9, 1988 - Unit 2 tripped from 20% power on low-low level in
June 9, 1988 - Unit 2 tripped from 20% power on low-low level in
                                        #2 steam generator due to feedwater heater isolations which
#2 steam generator due to feedwater heater isolations which
                                        caused feed flow and steam generator level transients.
caused feed flow and steam generator level transients.
                                        November 18,1988 - Unit 1 tripped from 72% power due to an
November 18,1988 - Unit 1 tripped from 72% power due to an
                                        electrical ground in the main generator which tripped the main
electrical ground in the main generator which tripped the main
                                        turbine.
turbine.
                                        December 26,1988 - Unit 1 tripped from 75 power on low-low
December 26,1988 - Unit 1 tripped from 75 power on low-low
                                        level in #4 steam generator. The trip was caused by a series of
level in #4 steam generator.
                                        events that started with a manual trip of the main turbine due
The trip was caused by a series of
                                        to generator seal rubbing. After the turbine trip, steam
events that started with a manual trip of the main turbine due
                                        generator level was controlled using manual feedwater control
to generator seal rubbing.
                                        which resulted in a feedwater isolation from high-high level in
After the turbine trip, steam
                                        #2 steam generator followed by the reactor trip on low-low *
generator level was controlled using manual feedwater control
                                                                                                      level
which resulted in a feedwater isolation from high-high level in
                                        in #4 steam generator.
#2 steam generator followed by the reactor trip on low-low level
                                I. Effluent Release Summary
*
                                                                1985           19.86         1987
in #4 steam generator.
                                  Gases                     (Curies)       (Curies)     (Curies)
I.
                                  Fission and Activation
Effluent Release Summary
                                  Gases                     4.57 E+03     1.21 E-00       0.0
1985
                                  Halogens and
19.86
                                  Particulate               6.63 E-03     1.56 E-03     5.04 E-04
1987
                                  Liquids
Gases
                                  Fission and Activation
(Curies)
                                  Products                   2.08 E 00     1.65 E-01     4.66 E-01
(Curies)
                                  Tritium                   6.33 E+02     1.72 E+02     1.19 E+02
(Curies)
                                J. Acronyms
Fission and Activation
                                  ALARA      -    As-Low-As-Reasonably-Achievable
Gases
                                  ASME        -     American Society of Mechanical Engineers
4.57 E+03
                                  ANSI        -
1.21 E-00
                                                    American National Standard Institute
0.0
                                  ANI        -
Halogens and
                                                    American Nuclear Insurer     *
Particulate
                                  AVO         -
6.63 E-03
                                                    Assistant Unit Operator
1.56 E-03
                                  AVT        -
5.04 E-04
                                                    All Volatile Treatment
Liquids
                                  CAQR        -     Condition Adverse to Quality
Fission and Activation
                                  CCW        -
Products
                                                  , Component Cooling Water
2.08 E 00
                                                                                      .
1.65 E-01
      , _ _ . _ . _ _ _ _ _
4.66 E-01
Tritium
6.33 E+02
1.72 E+02
1.19 E+02
J.
Acronyms
As-Low-As-Reasonably-Achievable
ALARA
-
American Society of Mechanical Engineers
ASME
-
American National Standard Institute
ANSI
-
American Nuclear Insurer
ANI
-
*
AVO
-
Assistant Unit Operator
All Volatile Treatment
AVT
-
Condition Adverse to Quality
CAQR
-
, Component Cooling Water
CCW
-
.
, _ _ . _ . _ _ _ _ _


                        _                           _                               _                                 _                                     .
,
                      ,                                                                                                                                          .
_
          -..
_
            .
_
  .
_
    !p .
.
    c                                             65-
.
                                                                                                                                                                    '
-..
                  CEG    -      Contract [ngineeringGroup.
.
.
!p .
c
65-
'
Contract [ngineeringGroup.
CEG
-
Nuclear Performance Plan
'
'
              ' NPP.-     -
' NPP.-
                                  Nuclear Performance Plan
-
                'DBVP      -      Design Easeline Verification Program
Design Easeline Verification Program
                  DNE.    -     Division of Nuclear Engineering
'DBVP
                  EA      -       Escalated Enforcement Action
-
                                  Emergency Core Cooling-System
Division of Nuclear Engineering
                              ~
DNE.
                  ECCS    -
-
                  ECP    -
Escalated Enforcement Action
                                ' Employee Concerns Program
EA
                .ECTG      -       Employee-Concerns Task Group
-
                  EDG    -       Emergency Diesel Generator
ECCS
                  E0P    -       Emergency Operating Procedures
~
                  EP      -
Emergency Core Cooling-System
                                  Emergency Preparedness
-
L                  EPRI.  -
' Employee Concerns Program
                                  Electric Power Research Institute
ECP
                  EQ      -
-
                                  Environmental Qualification
Employee-Concerns Task Group
                  ERCW    -     ' Essential Raw Cooling Water
.ECTG
        ,        FT      -
-
                                  Flow Transmitter
Emergency Diesel Generator
                :GET.      -       General Employee Training
EDG
                  GL      -       Generic Letter
-
                  HP      -       Health Physics
Emergency Operating Procedures
                  IDI    -       Integrated Design Inspection
E0P
                  INP0    -       Institute for Nuclear Power Operations
-
                  IR-     -      Inspection Report..
Emergency Preparedness
                  ISEG    -     Independent Safety Engineering Group
EP
                  ISI.    -     Inservice Inspection
-
                  IST      -   ' Inservice Testing
Electric Power Research Institute
                  LC0    -       Liraiting Cordition'for Operation
L
                  .LER
EPRI.
                          -       Licensee Event Report
-
                  'MIC    -       Microbiologically Incuced Corrosien
Environmental Qualification
                  MILES   -
EQ
                                  Multiple Integrated Laser Engagen.ent System
-
                  MOVAT    -      Motor Operated Valve Actuators
' Essential Raw Cooling Water
                  MSIV    -
ERCW
                                  Main Steam Isolation Valve
-
                  NMRG     -     Nuclear Maintenance Review Group
Flow Transmitter
                  NOUE    -
FT
                                  Notice of Unusual Event
-
                  NRC      -     Nuclear Regulatory Commissior..
,
                .NRR      -     Nuclear Reactor Regulation
General Employee Training
                  NSRB    -     Nuclear Safety Review Board
:GET.
                  OPDT    -     Over Power Delta Temperature
-
                  OSP      -     Office of Special Projects
Generic Letter
                  OTDT    -     Over Temperature Delta Temperature
GL
                  PM      -
-
                                  Preventive Maintenance
Health Physics
                  PMT      -     Post Modification Testing
HP
                  PORC    -     Plant Operations Review Ccmaittee
-
                  PWR      -     Pressurized Water Reactor
Integrated Design Inspection
                  QA      -     Quality Assurance
IDI
                  QMDS    -     Q6alified Maintenance Document System
-
                  QVI      -     Ouality Verification Inspection
Institute for Nuclear Power Operations
                  RII      -
INP0
                                  Region II
-
                  RCA      -
Inspection Report..
                                  Radiation Centrolled Area
IR-
                  RCS      -     Reactor Coolant System
-
                  RHR       -
Independent Safety Engineering Group
                                  Residual Heat Removal
ISEG
                  RIP      -     Replacement Items Program
-
                                                          . _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ - - _ _ _ - _ _ _ _ _ - - _ _ _ _ _ _ _ - _ _ _ _ _ _ _ _ _ _ _ -
Inservice Inspection
ISI.
-
' Inservice Testing
IST
-
Liraiting Cordition'for Operation
LC0
-
Licensee Event Report
.LER
-
Microbiologically Incuced Corrosien
'MIC
-
MILES
-
Multiple Integrated Laser Engagen.ent System
Motor Operated Valve Actuators
MOVAT
-
Main Steam Isolation Valve
MSIV
-
NMRG
-
Nuclear Maintenance Review Group
Notice of Unusual Event
NOUE
-
Nuclear Regulatory Commissior..
NRC
-
Nuclear Reactor Regulation
.NRR
-
Nuclear Safety Review Board
NSRB
-
Over Power Delta Temperature
OPDT
-
Office of Special Projects
OSP
-
Over Temperature Delta Temperature
OTDT
-
Preventive Maintenance
PM
-
Post Modification Testing
PMT
-
Plant Operations Review Ccmaittee
PORC
-
Pressurized Water Reactor
PWR
-
Quality Assurance
QA
-
Q6alified Maintenance Document System
QMDS
-
Ouality Verification Inspection
QVI
-
Region II
RII
-
Radiation Centrolled Area
RCA
-
Reactor Coolant System
RCS
-
RHR
Residual Heat Removal
-
Replacement Items Program
RIP
-
. _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ - - _ _ _ - _ _ _ _ _ - - _ _ _ _ _ _ _ - _ _ _ _ _ _ _ _ _ _ _ -


    ( ,.                           .       _         _                   - _ _ _ _ _ _ _ _ . _ _ _ - . - _ .   _______ _
( ,.
    ff jr , y
.
            ' ''
_
        ;4
_
        j
- _ _ _ _ _ _ _ _ .
        .c     '
_ _ _ -
                                                                66;
. - _ .
      ,
_______ _
                          RTD-         --     Resistance Temperature Device
ff jr , y
                          SALP.:      -      Systematic Assessment of Licensee Performance
' ''
                          SG0G-       -      Steam Generators Owners Group
;4j
                          SI'          --     Surveillance Instruction
.c
      .                  SNPP        -     Sequoyah Nuclear Performance Plan
66;
                        . 501            .
'
                                              System Operating Instruction-
,
                        ' TACFs
Resistance Temperature Device
                        .
RTD-
                                        -
--
                                              ' Temporary Alterations
Systematic Assessment of Licensee Performance
                        ' TDAFW-       -      Turbine Driven Auxiliary Feedwater Pump
SALP.:
                          TS             .   Technical Specifications
-
                          TSCR        -      Technical Specification Change Request
Steam Generators Owners Group
                          TVA'        -     Tennessee Valley Authority
SG0G-
                          TVAPD       -    'TVA Projects Division (NRC)
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                          UHI          -       Upper Head Injection
Surveillance Instruction
                          VCT-         -      Volume' Control Tank
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Sequoyah Nuclear Performance Plan
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System Operating Instruction-
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' Temporary Alterations
' TACFs
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Turbine Driven Auxiliary Feedwater Pump
' TDAFW-
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Technical Specifications
TS
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Technical Specification Change Request
TSCR
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Tennessee Valley Authority
TVA'
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TVAPD
'TVA Projects Division (NRC)
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Upper Head Injection
UHI
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VCT-
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Latest revision as of 03:17, 2 December 2024

SALP Repts 50-327/89-01 & 50-328/89-01 for 880204 - 890203
ML20245B717
Person / Time
Site: Sequoyah  Tennessee Valley Authority icon.png
Issue date: 02/03/1989
From:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML20245B703 List:
References
50-327-89-01, 50-327-89-1, 50-328-89-01, 50-328-89-1, NUDOCS 8904260238
Download: ML20245B717 (68)


See also: IR 05000327/1989001

Text

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ENCLOSURE 1

INTERIM SALP REPORT

U. S. NUCLEAR REGULATORY COMMISSION

OFFICE OF NUCLEAR REACTOR REGULATION

SYSTEMATIC ASSESSMENT OF LICENSEE PERFORMANCE

,

NRC INSPECTION REPORT NUMBER

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50-327/89-01 AND 50-328/89-01

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TENNESSEE VALLEY AUTHORITY (TVA)

SEQUOYAH NUCLEAR PLANT, UNITS 1 AND 2

FEBRUARY 4, 1988 - FEBRUARY 3, 1989

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TABLE OF CONTENTS

PAGE

I.

INTRODUCTION..................................................

-1

A.

Licensee Activities.....................................

2

B.

Direct inspection and Review Activities.................

5

i'

II.

SUMMARY OF RESULTS...........................................

7

A.

Basis Period Summary....................................

7

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B.

Assessment Period Summary..............................

17

C.

0verview...............................................

18

Ill. CRITERIA....................................................

19

IV.

PERFORMANCE ANALYSIS........................................

20

.

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A.

Plant 0perations.......................................

20

.

B.

Radiological

Controls..................................

27

C.

Maintenance / Surveillance...............................

30

D.

Emergency Preparedness.................................

39

E.

Security...............................................

40

F.

Engi.neering/ Technical. Support..........................

42

G.-

Safety Assessment /Quali ty Verification. . . . . . . . . . . . . . . . . ., 48

V.

SUPPORTING DATA AND SUMMARIES...............................

54

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A.

Investigation Review...................................

54

B.

Escalated Enforcement Action...........................

55

C.

Management Conferences.................................

55

D.

Confirmation of Action Letters.........................

56

E.

Review of Licensee Event Reports.......................

57

F.

Licensing Activities...................................

57

G.

Enforcement Activity...................................

63

H.

Re a c t o r T r i p s . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . .

6 3

I.

E f fl u e nt R el e a s e S umm a ry . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . .

64

J.

Acronyms...............................................

64

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I.

INTRODUCTION

The Systematic Assessment of Licensee Performance (SALP) program is an

integrated NRC staff effort to collect available observations and data on

a periodic basis and to evaluate licensee performance on the basis of this

information.

The program is supplemental to normal regulatory prococses

used to ensure compliance with Nuclear Regulatory Commission rules and

regulations.

It is intended to be sufficiently diagnostic to provide a

rational basis for allocating Nuclear Regulatory Commission (NRC)

resources and to provide meaningful feedback to the licensee's management

regarding the NRC's assessment of their facility's performance in each

functional area.

l

)

The last SALP appraisal period for Sequoyah was for the period

l

March 1,1984 through May 31, 1985 with the SALP report being issued on

September 17, 1985.

In August 1985, both units were shutdown for Environ-

mental Qualification (EQ) verification.

In the September 17, 1985 letter

j

transmitting the TVA SALP reports, the NRC communicated that significant

programmatic and management deficiencies existed in TVA's nuclear program

and pursuant to 10 CFR 50.54(f), TVA was requested to address these de-

ficiencies prior to the s'tartup of any nuclear unit.

TVA responded by

issuing and implementing the Corporate and Sequoyah Nuclear Performance

Plans.

NRC evaluation of the performance plan implementation is docu-

mented in NUREG-1232, Volumes 1 and 2, respectively, and NRC inspection

reports.

Furtier SALP review was deferred pending restart of Unit 2.

By

letter dated May 26, 1988, TVA was notified that the normal SALP evalua-

tion process had recommenced as of February 4,1988.

An NRC SALP Board, composed of the staff member s listed below, met on

flarch 28, 1989, to review the observations and data on performance, and

to assess licensee performance in accordance with Chapter NRC-0516,

" Systematic Assessment of Licensee Performance." The guidance and evalo-

ation criteria are summarized in Section III of this report.

The Board's

findings and recommendations were forwarded to the Associate Director for

Special Projects, Office of Nuclear Reactor Regulation, for approval and

issuance.

This report is the NRC's assessment of the licensce's safety performance

at Sequoyah for the period February 4,1988 through February 3,1989.

The SALP Board for Sequoyah was composed of:

B. D. Liaw, Director, TVA Projects Division (TVAPD), Office of

fluclear Reactor Regulation (NRR) (Chairman)

L. J. Watson, Acting Assistant Director for Inspection Programs,

TVAPD, NRR

S. C. Black, Assistant Director for Projects, TVAPD, flRR

R. C. Pierson, Assistant Director for Technical Programs, TVAPD, NRR

D. M. Collins, Chief, Radiological Protection and Emergency

Preparedness Branch, Region II (RII)

A. F. Gibson, Director, Division of Reactor Safety, RII

J. N. Donohew, Senior Project Manager, TVAPD, NRR

K. M. Jenison, Senior Resident Inspector, TVAPD, NRR

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The following staff also attended the Sequoyah SALP Board meeting:

J. Brady, TVF D, NRR

P. Harmon, TVAPD, NRR

,

G. Hubbard, TVAPD, NRP,

S. Weiss, TVAPD, NRR

B. Zalcman, Technical Assistant, NRR

E. Goodwin, TVAPD, NRR

B. Desai, TVAPD, NRR

K. Landis, RII

R. Borchardt, RII Coordinator, ED0

T. Rotella, TVAPD, NRR

A.

Licensee Activities

Both units began the assessment period in shutdown from an extended

outage that began in August 1985.

TVA agreed, in 1985, not to

restart the units without receiving NRC approval.

On February 4,1988, Unit 2 received NRC permission to enter Modes 4

I

and 3 (hot shutdown and hot standby) and began the heatup process.

The plant was heated up using reactor coolant pump heat and entered

l

Mode 4 on February 6,1988.

While in Mode 4, approximately nine

i

personnel errors occurred which included inadvertent Main Steam

Isolation Valve (MSIV) closures and feedwater isolations, generation

of a reactor trip signal, and a loss of Volume Control Tank (VCT)

level.

None of the events resulting from those personnel errors

represented significant safety concerns of their own accord and

collectively appeared to be typical of what one would expect of a

near term operating plant going through the same evolution.

On February 27,1988, Unit 2 entered Mode 3.

While in Mode 3, a

number of events occurred including inadvertent closure of all four

MSIVs, exceeding Technical Specification (TS) surveillance limits for

Reactor Coolant System (RCS) leakage, exceeding RCS cold leg accumu-

lator boron concentration, and two events involving auxilicry

feedwater pump operability and charging pump operability of which the

later involved escalated enforcement.

The majority of these events

were personnel related and were responded to by the licensee in an

l

adequate manner.

On March 22, 1988, the NRC Commissioners voted to allow Unit 2 to

restart. On March 30, the NRC approved entry into Mode 2 (Startup).

On March s1, prior to actually beginning dilution, the licensee

determined that modifications would be required on one of the three

pressurizer safety valve loop seals, and the restart was delayed.

During resolution of problems with pressurizer loop seals, a tube

leak was identified in the #3 steam generator.

On April 7, Unit 2

began a cooldown to Mode 5 (cold shoutdown) to repair the steam

generator tube leak and complete pressurizer loop seal modifications.

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On May' 7', Unit 2 began the heatup process again and entered Mode. 4.

On May 11, Unit 2 entered Mode 3 and on May 12, Unit 2 entered Mode 2.

Control rods were withdrawn and dilution to criticality Began.

On

May 13, the reactor achieved criticality, entered Mode 1 (power

operation), and the generator was synchronized with the grid.

On May

15, the NRC granted permission to allow operation above 30% power and

.

power escalation was resumed.

During the power escalation process

several minor events occurred which included the discovery of an

unqualified splice in the circuitry for one of the steam generator

water level indicators.

On May 19, Uni

2 tripped from 73% power due to steam flow / feed flow

mismatch coincident with low-low steam generator level.

This situa-

tion occurred due to maintenance being performed concurrently cn two

pieces of equipment which together could cause a reactor trip (one

channel of steam generator level indication to replace the

unqualified splice and the #3 heater drain tank level controller

which resulted in plant oscillations).

On May 20, efter corrective

actions for the trip were completed, NRC permission was given to

restart Unit 2.

On May 21,' Unit 2 achieved criticality. entered Mode 1, and was

synchronized with the grid.

.

On May 23, Unit 2 tripped from 70% power on low fbs in RCS Loop #4.

This occurred due to a personnel error while performing a surveil-

lance instruction on the loop #4 flow transmitters.

Or, May 24, Unit

2 achieved criticality, synchronized with the grid and began power

escalation.

1

On May 24, while Unit I was in partial drain to plug steam generator

tubes, a loss of decay heat removal occurred due to an cperatcr error

,

in positioning valves while changing the residual heat removal (RHR)

system alignment.

On May 29, 1988, Unit-2 achieved 100% reactor power.

On June 6,1988, Unit 2 tripped from 98% power on stean flow / feed

flow mismatch coincident with low level in #4 steam generator. The

.

trip occurred while performing a surveillance on the feedwater

l

regulating valves and resulted because a diode was missing in the

block circuit.

On June 8,1988, Unit 2 tripped from T2% power on low-low level in #2

steam generator.

The trip was caused by operator error when placing

the feed pump contro'.ler in the automatic position which resulted in

i

steam generator level oscillations.

On June 9, 1988, Unit 2 tripped from 20% power on low-low level in 72

steam generator.

The trip was caused by transients in feed flow and

steam generator level which were initiated by feedwater heater

isolations.

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'On June 13, 1988, TVA mec with the NRC staff to discuss the root

causes _ for the five reactor trips which had occurred since Unit 2

restarted on May 18, 1988.

Corrective actions identified included

l

reducing the number of outstanding secondary plant work requests

which could contribute to balance of plant induced reactor trips.

On June.19, 1988, the NRC granted permission t'o restart Unit 2.

On

June 30,1988, Unit 2 reached 70% reactor power (holding for core

life extension).

On September 27, 1988, the NRC granted permission ~for Unit I to enter

Mode 4.

While in Mode 4, several unanticipated reactor trip signals

were gener M due to personnel

errors while performing

surveillance.

On October 20, 1983, Unit 1 entered Mode 3.

While in Mode 3, the UHI

membrane was ruptared while putting the system in service due to.

improperly labeleo valves.

Equipment problems such as steam

generator safety valve at leakage, pressurizer safety valve seat

, leakage, reactor vessel inner seal leakage, and steam dump packing

leakage were encountered and properly resolved.

On ' November. 6,1988, Unit 1 entered Mode 2 and went critical .

On

November 10, 1988, Unit 1 entered Mode

1,

the generator was

synchronized with the grid, and power escalation began.

Several

personnel errors related to equipment surveillance

caused ESF

actuations while in Modes 2 and 1.

On November 18, 1988, Unit 1 tripped from 72% power due to an

electrical ground in the main generator stator.

During the forced

outage to repair the generator stator, repairs to leaking steam

generator safety valves and a pressurizer safety valve were also

accomplished.

,

On December 25,1988, Unit 1 achieved criticality, entered Mode 1,

the generator was synchronized with the grid, and power escalation

began.

On December 26,1988, Unit 1 tripped on low-low level in #4 steam

generator.

The trip was caused by a series of events that started

with a manual trip of the turbine due to generator seal rubbing.

After the turbine trip, steam generator level was controlled using

manual feedwater control which resulted in a feerwater isolation from

high-high level in #2 steam generator followed by the reactor trip on

low-low level in #4 steam generator.

On December 27,1988, Unit 1 achieved criticality and began power

escalation.

On December 30, 1988, Unit I achieved 98% reactor power.

On January 19, 1989, Unit 2 was shutdown to begin the s heduled cycle

3 refueling outage after 210 continuous days of operation.

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B.

Direct-Inspection and Review Activities

During the assessment period, routine inspections were performed at

the Sequoyah facility by the NRC. staff.

Special inspections were

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conducted as follows.:

February 4~- June 25, 1988; a series of special inspections.cf

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the Unit 2 heatup and restart effort were conducted by the NRC

Sequoyah Restart Task Force.

These inspections included control

room observation and reviews of activities associated with the

restart effort. (88-02,88-17,88-20,88-22,88-26,88-28,88-34)

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February 1-19, 1988; a special inspection was performed to

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assess the corrective actions performed by TVA in response to

the findings of the Integrated Design Inspection. (88-13)

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February 8-12, 1988; a special inspection was conducted to

assure that the licensee's corrective action program implementa-

tion adequately dispositioned adverse conditions, including

generic issues. (88-15)

February 15-19, 1988; a special inspection of the open restart

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issues' in the civil engineering area was conducted to determine

that adequate corrective action and resolution had occurred to

support the restart of Unit 2. (88-12)

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February 29 - March 4, 1988; a special operational readiness

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inspection was conducted to assess the adequacy of the

licensee's preparations for Unit 2 restart. (88-16)

March 14-23, 1988; a special fire protection inspection was

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conducted for Unit 2 restart in the area of implementation of

the' requirements of 10 CFR 50 Appendix R, Sections III.G, III.J.

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III.L, and 111.0 including safe shutdown logic. (88-24)

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June 20 - July 8,

1988; a special Safety System Quality

Evaluation vertical slice review was conducted on the

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Containment Spray System to assess the licensee's Nuclear

Performance Plan implementation for Unit I restart. (88-29)

July 11-15 and August 23-24, 1988; a special inspection was

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conducted to assess the effect of excessive cooldowns following

reactor trips on end-of-life shutdown margin. (88-35)

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' July 25-28, 1988; a special fire protection inspection was

conducted for Unit 1 restart in the area of implementation of

the requirements of 10 CFR 50 Appendix R, Sections III.G, III.J,

III.L, and 111.0 including safe shutdown logic. (88-37)

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August 29 - September 2,1908; a special operational readiness

inspection was conducted to assess the adequacy of the

licensee's preparations for Unit 1 restart. (88-42)

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September 6-9, 1988; a special inspection was conducted to

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assess the licensee's unreviewed safety question determination

program and implementation. (88-43)

September 25 - November 21, 1988; a series of special inspec-

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tions of the Unit I heatup and restart effort were conducted by

the NRC Sequoyah Restart Task Force.

These inspections included

control room observation and reviews of activities associated

with the restart effo-t. (88-40,88-46,88-47,88-48,88-49,88-51,

88-52,88-55)

December 12, 1988 - January 26, 1989; a special ' quality

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verification inspection was conducted in the areas of

maintenance, modifications, operations, radwaste processing, and

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correctiveactions.(88-50)

The staff spent more effort on Sequoyah than on any other operating

plant and also expended more effort than 'during the basis period.

Reviews by the staff included TVA's Corporate and Sequoyah Nuclear

Performance Plan (NPP) programs; the Employee Concern Task Group

(ECTG) element reports; sixty-five amendments to the Unit 1 and 2

Technical Specifications including an exigent amendment, an emergency

amendment, and a waiver of compliance; and four exemptions.

The NPP

reviews were documented in the NRC Safety Evaluation Report

NUREG-1232 Volume 1 and 2 and its supplement, and included reviews in

the major areas of adequacy of design, special programs, restart

readiness, employee concerns, and allegations.

The areas of adecuacy

of design, special programs, and restart readiness were further

. broken down as follows:

Adequacy of Design

1.

Plant Modification and Design Control

2.

Design Baseline Verification Program

3.

Design Calculations Program

4.

Alternately Analyzed Piping and Supports

5.

Cable Tray Supports

6.

Concrete Quality

7.

Miscellaneous Civil Engineering Calculations

Special Programs

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Fire Protection

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2.

Environmental Qualification of Electrical Equipment

Important to Safety

3.

Piece Part Qualification (Procurement)

4.

Sensing Line Issues

5.

Welding

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Containment Isolation

7.

Contair, ment Coatings

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Moderate-Energy Line Breaks

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ECCS Water Loss Outside Crane Wall / Air Return Fan

0perability

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10.

Platform Thermal Growth

11.

Pipe Wall Thinning Assessment

12.

Cable Installation

13.

Fuse Replacement

Restart Readiness

1.

Operational Readiness

2.

Management

3.

Quality Assurance

4.

Operating Experience Improvement

5.

Post-Modification Testing

6.

Surveillance Instruction Review

7.

Operability "Look Back"

8.

Maintenance

9.

Restart Test Program

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Training

11. Security

1~2 .

Emergency Preparedness

13.

Radiological Controls

14.

Restart Activities List

II. . SUMMARY OF RESULTS-

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' A' comparison of the present SALP ratings to the previous SALP ratings cf 4

years ago (1984 to 1985) would be of little benefit in determining the

current trend of the licensee.

In order to evaluate the current trend cf

the licensee from the

reassessment period to the assessment period, an

additional summary is provided below of the NRC staff evaluation for the

period from January 1,1987 until the start of the assessment period

(February 4,1988) to be used as a basis for comparison.

The' NRC established an Office of Special Projects (0SP) in February 1987

to address the particularly complex regulatory problems of TVA and one other

utility.

Part of the OSP goal was to assess whether identified problems

to the licensee were on a path to an acceptable solution, and where not,

to identify acceptable solutions necessary to enable the staff to complete

its licensing reviews of these facilities, consistent with the NRC's

statutory mandate to protect the health and safety of the public.

A.

Basis Period Summary (January 1,1987 - February 3,1988)

1.

Plant Operations

During the entire basis period both units were in the shutdown

mode.

Weaknesses were identified in the adequacy of Abnormal

and Emergency Operating procedures, emergency contingency action

procedures, compensatory operator actions,

configuration

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control, the clearance process, investigation and resolution of

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event related issues, . involvement of first line and upper level

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management in the day-to-day operation of the plant, and control

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and authority over plant activiMes impacting schedule. Some

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deportability / operability determinatices were classified as

unknown while awaiting Division of Nut ear Engineering (DNE)

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review which was not always t;mely or responsive.

In addition,

there was a reluctance by the licensee to report items that they

felt were minor.

As a result, several events were nct properly

classified and repneted.

Material condition, drawing adequacy

and configuration management training were acceptable.

These issues indicated a lack of management attention to and

involvement in the operational aspects of the plant.

Control

room operators were burdened with the work control management

function.

Their decisions in controlling these activities were

often reversed by management.

This resulted in limiting the

amount of time senior reactor operators spent in the plant, a

reduction in the amount of time reactor operators spent

observing control panel indications, and a feeling that

management did not respect their ability to make decisions.

Several management changes occurred during the basis period

which contributed to major improvements.in plant activities. The

new managers included the Deputy Site Director, Plant Manager,

Operations Superintendent, and Corporate Outage / Maintenance

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Managers.

The operations section was adequately staffed to suppnrt piant

operations. ' Control room and plant shif t rotation was increased

to a six shift rotation late in the basis period.

Overtime wcs

routinely used to augment normal shift staffing with several

occasions identified where administrative limits were exceeded

without receiving prior plant manager approval.

The 1987 i;RC

replacement examinations for licensed operators indicated

satisfactory results (5 out of 5 passed).

Measures were implemented to revise and control primary drawings

in the control room.

These drawings were redrawn and

maintained by computer-aided drafting systems which resulted in

improved accuracy and a more timely revision process.

System

logic drawings.were removed from the primary drawing list during

1986 because they were not routinely updated and revised as

plant systems were modified.

Procedural compliance by Operations personnel was judged to be

marginally better than the plant staff as a whole.

Instances of

procedure deviations and non-compliances occurred at an

unacceptable frequency, and resulted in several reportable

events.

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.The licensee made considerable progress in resolving the several

hundred technical issues encountered after the 1985 shutdown of

both units.

Issues that remained to be resolved at the end of

the basis period included the evaluation of containment sump

level transmitters, lower containment coolers, and Senior

Operator manning.

2.

Radiological Controls

Inspections conducted during the basis period of the Sequoyah

radiation protection program, indicated that the actions taken

by the licensee, including correction of previous weaknesses in

its program for maintaining exposure as-low-as-reasonably-

achievable (ALARA), were sufficient to support plant restart.

One significant event involved an exothermic reaction during a

radwaste solidification process which caused personnel

contaminations and higher than expected radiation levels.

Considerable organizational changes had taken place in the

Chemistry Group during the period.

These revisions assured

close management involvement in maintenance of quality, storage

of radioactive waste, and effluent releases.

Close coordination

with the Corporate Chemistry group resulted in resolution of

. technical issues in a timely manner.

The organizations were responsive to NRC initiatives in that

open items were being . closed out as the organization prepared

,,

for Unit 2 startup.

Staffing had been reviewed, and several new

management personnel were added to the Chemistry Group.

3.

Maintenance / Surveillance

During the SALP basis period the Sequoyah maintenance program

experienced numerous weaknesses.

These weaknesses were in

procedural

compliance,

corporate maintenance

guidcnce,

maintenance trending, root cause analysis, first line manage-

ment involvement, training for maintenance planners, work

control, maintenance coordination, equipment classification

(Q-list), maintenance history tracking and trending, mainten-

ance procedure adequacy, plant drawing use, the preventive

maintenance program, accountability of maintenance tools and

equipment, post modification testing, quality assurance

involvement with maintenance activities, temporary alterations,

and corrective action.

In addition, there were significant

backlogs .in the modifications, temporary modifications, and

maintenance areas.

There was significant overlap between those

issues identified by ,the NRC and those issues identified by

TVA's Nuclea.r Manager's Review Group maintenance inspections.

Tracking, trending and scheduling were improved and craft

reviews were implemented which improved the quality of mainten-

ance activities. Areas that did not demonstrate active direction

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during the basis period were the maintenance instruction

enhancement project which was resolved during the SALP

assessment period,' and composite maintenance crews which were

identified by the Nuclear Maintenance Review Grcup (NMRG) as

having implementation problems but were not acted upon by TVA

. management.

Institute for Nuclear Power Operations (INP0)

accreditation of the training for nine previously selected

maintenance craft areas was received during the SALP basis

period.

The NRC identified significant problems in the area of procure-

ment of safety-related parts and equipment at Sequoyah and was

'

considering escalated enforcement action.

Based on the NRC

findings, TVA in general and Sequoyah in particular initiated an

extensive Replacement Items Program (RIP) to ensure that

appropriate parts and equipment were installed in the plant for

EQ and seismic qualification of equipment prior to the restart

of the Sequoyah units.

This included training in repair part

and procurement control which was considered one of the causes

.

of the problem.

Based on the shutdown plant enforcement policy

I

and successful implementation prior to unit restart, these

issues were given discretionary enforcement.

The program also

established controls to ensure that future procurement of

safety-related equipment met the appropriate requirements.

Sequoyah was completing the documentation and field work for ,

their EQ program.

Sequoyah was found to have an excellent EQ

program which had proper management attention ard proposed sound

technical resolutions as problems arose.

TVA management was

found to be knowledgeable of NRC and industry standards and

requirements in this area.

Licensee management recognized that storage of equipment did not

-meet the requirements of American National Standard Institute

(ANSI) 45.2.2 and initiated an improvement program to correct

this problem.

The' equipment storage upgrade program initiated

by licensee management was adequate and well implemented.

The

implementation included a computerized tracking system to

,

i

identify the exact location of each part, and well organized,

clearly marked storage areas that met the ANSI 45.2.2 storage

class requirements, even at remote on-site locations.

At the

close of the SALP tasis period safety related component storage

was in excellent condition, as a result of several energetic

knowledgeable managers who were personally involved in the

resolution of this industry wide issue.

As a resul t of significant NRC concerns with surveillance

instruction inadequacies which were under consideration for

escalated enforcement, the licensee established a surveillance

instruction review team to compare existing surveillance

i

instructions to TS surveillance requirements.

This review

1

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11

effort identified.a significant number of additiona! issues that

resulted in approximately 15 Licensee Event Reports (LERs) being

written.

A number of significant revisions and management

changes were inade to' the surveillance instruction review and

update program to achieve technically adequate surveillance

instructions that met the surveillance requirements. Management

involvement in the final effort was aggressive and included an

independent validation process which wcs particularly well

l

managed and ensured that the surveillance instructions produced

were of high quality and technically adequate.

Based on the

shutdown plant enforcement policy and implementation of an

acceptable surveillance program prior to restart, these issues

i

were given discretionary enforcement.

The licensee established a Nuclear Performance Plan Restart Test

Program in order to ensure the operability of scfety related

,

equipment which had been modified.

A review matrix of component.

i

functions and previous",y performed surveillance was established

'

to ensure the testing of functions that had not been tested.

This program was considered adequately staffed with trained

individuals and was determined to be acceptable.

Only the

closure of Mode 3 and 2 related items was deferred into the SALP

period.

A problem was identified in the Inservice Test (IST) valve test

program in that essentially all category A and B valves were

~ included in one Surveillance Instruction (SI) and scheduling was

. based on the issue date for the SI package, not the test date

for individual valves in the package.

The test dates for

individual valves were not controlled resulting in a number of

valves exceeding their. test frequency.

,

i

Procedural adherence was a weakness which contributed to several

!

'

events and enforcement actions and indicated a lack of manage-

ment involvement in and attention to this area.

In addition,

corrective actions were not effective in reducing the results of

this weakness until well into the SALP assessment period.

!

Conduct of testing was identified as an area of weakness during

the activities leading up to the restart of Unit 2.

The

licensee took strong corrective action with the issuance of

special conduct of testing administrative controls which

resulted in a significant improvement in plant operations.

The effectiveness of the short term layup of the steam and power

conversion system (the secondary water system) was adversely

affected due to uncertainties in the startup schedule.

The

uncertainties were directly related, to the inability of

management to control restart activity schedules.

Continuous

maintenance and modifications of systems created a condition

where the desired controls did not in some cases maintain the

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parameters for minimizing corrosion and degradation of the

car1 steel systems.

The licensee was responsive to NRC

cor

ms expressed during inspections and to NRC information

not

a.

Actions were taken to enhance the pro,tection of

systems .during the extended short term layup.

Organizational changes in the water chemistry program were a

strengthening factor for water chemistry control.

Qualifica-

tions of the chemistry management and staff were adequate with a

sufficient number of chemists and analysts to maintain chemistry

control.

Other elements of the water chemistry progran

(procedures, training, and equipment) were maintained at a

'

sufficient level to achieve chemistry control during plant

startup.

During the basis period the licensee made progress in changing

its maintenance philosophy from reactive to preventive and was

trying to reinforce procedural compliance.

4.

Emeroency Preparedness

The Emergency Preparedness program was adequately maintained

during the basis period.

Two routine inspections and an

emergency exercise indicated the. licensee was maintaining an

effective emergency preparedness program.

Licensee management

attention to the program was adequate

The two violations

-

identified during the rcutine inspections oddressed an

inadequacy in the training for licensed operators and a failure

to conduct required monthly concunications checks fcr three

months.

5.

Security

Four routine' security inspections, one material control

'

inspection and two special inspections relative to Fitness for

Duty and pre-employment screening were conducted.

Two

violations were tited for failure to adequately post a

compensatory officer, and for failure to maintain a bullet-

resistant barrier.

The Fitness for Duty program was judged

adequate with both a few noteable strengths and one significant

weakness.

The NRC exercised discretionary enforcement in not

issuing a violation regarding numerous pre-employment screening

errors due to the significant corrective action initiated and

that the program was examined and determined acceptable prior to

plant startup.

During this period the licensee, although

non-operational, did not reduce its security program nor did it

"de\\ italize" any of its security areas.

The NRC inspection

proc, ram also included various allegations, Employee Concerns and

the licensee's Regulatory Improvement Plan.

I

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A licensee Quality Assurance -Audit (QSS-A87-0010) was

performed and no regulatory issues were raised. With respect to

Safeguards Event Reports, there were four relative to expired

!

badges not being voided and various visitor / escort deficiencies.

7_

Of the 225 security incident reports per 10 CFR 73.71

n

requirements, the vast majority (nearly 95%) resulted from the

failure of equipment (hardware and systems) and not human

errors.

Midway through this period, the licensee reorganized its

security organization which resulted in security officers

working for and being accountable to ,the Corporate Nuclear

Security Support Branch, as oppose to the previous multi-

management-level structure criticized in prior SALP Reports. A

new site Security Manager was assigned to the site in July 1987.

L

The extended' use of numerous compensatory iaeasures neeGd

!

because of failed equipment remained the. most significant

l

regulatory issue throughout this period.

ticwever, the licensee

was judged as adequately meeting requirements and providing

security for the facility.

-

6.

Engineering / Technical Support

The licensee's performance in the engineering / technical support

area was greatly affected by the many changes which were being

experienced by the engineering / technical support staff.

Early

in the baseline perind, the licensee was trying to obtain a

clear definition of the scope of effort required to resolve many

technical and design issues which had been identified through

licensee sponsored evaluations and audits and NRC inspections;

however, the engineering and technical support staff was

hampered by changes in organization structures and changes in

key personnel as well as major changes to the internal

engineering procedures.

While the above changes hampered early baseline period

performance in engineering / technical support, the licensee had

- established many special programs to address and resolve

previously identified issues as well as new issues identified

durug the baseline period (e.g. discrepancies identified during

the NRC integrated design inspectn (IDI)).

Some of the issues

for which special programs had two established included EQ of

safety-related electrical equipt ~t; design and configuration

control

(design baseline verification program);

design

calculations review - electrical, mechanical, nuclear, and

civil; electrical

issues; instrument sense line issues;

component and piece part qualification; Appendix R; and restart

testing.

_ - _ --

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The licensee performance in the - engineering / technical support

area was satisfactory for some of the programs; however, other

programs. were satisfactory only after corrections were made

based on NRC input.

Examples of programs where the licensee's

. performance was satisfactory and the program implementation was

considered acceptable were:

EQ; civil calculations; cable tray

supports; technical drawings; Design Baseline and Verification

Program (DBVP); and heat code traceability.

Examples of programs where program implementation was initially

considered inadequate included:

component and piece part

qualification (inadequate seismic qualification and dedication

of commerciti grade parts for use in safety .c

ted equipment);

pipe hangers and supports (inacecuate ~ caic i tions and

d

documentation to demonstrate that installed pipe hangers and

supports met plant design criteria); and instrument sense lines

and instrumentation accuracy calculations (lack of sufficient

conservatism).

While the licensee's implemen :ation of some

programs was initially judged to be unsatisfact'ry or inadequate

relative to engineering / technical support, once problems or

concerns were identified, the licensee satisfactorily resolved

the problems and completed the programs.

7.

Safety Assessment /Qu'ality Verification

For the basis period, there was an extensive review effort on

Sequoyah.

The review effort included the following significant

items:

.

1.

review of the Corporate Nuclear Performance Plan was

completed and NUREG-1232, Volume 1 was issued;

2.

most of the review of the Sequoyah Nuclear Performance Plan

was completed;

3.

most of the Employee Concerns Task Group (ECTG) element

reports on Sequoyah were reviewed;

4.

thirty amendments to the Units 1 and 2 TS were issued; and

5.

twenty-one meetings were held with TVA on various technical

issues.

Overall, the work submitted by TVA was reasonably good.

The

submittals generally showed evidence of prior planning by

management.

An understanding of the technical issues was

generally !pparent.

The resolutions of issues were generally

viable, timely, sound and well thought out with conservatism

exhibited by the licensee's approach.

This was generally true

in the basis period except for the issues of cable testing and

the transition of senior nuclear power management from contract

employees to permanent employees.

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-TheLissue of. cable testing which included the issue of-test ng

10'CFR 50.49 silicone rubber insulated cable which was inside

!"

containment ; was protracted and- drawn out.

.The issue' was -

discussed tnroughout the basis period and was not resolved for

L

'1

Unit 1 until the! staff letter of- May 25,.1988 in the . rating

period. ' Die resolution of this issue was not timely and -the

technical issues were not well thought out.

2 .

E

The TVA response to the staff's concer.:s on the transition of

TVA senior nuclear management was acceptable and the_ safety

,

- evaluation on the TVA's Corporate Nuclear Performance Plen was

issued on July 28, 1987; but, TVA was not responsive to the

issues raised ~ by the staff pertaining to the transition from

l

Jcontract managers to.TVA permanent managers.

As a result, the-

,

staff was compelled to request TVA to notify the staff 30 days-

<

in advance 'of any permanent changes of the senior nuclear

managers.

..

6

. In Janaery 1987, the NRC approved (for a period of two years)

.TVA's Quality Assurance Topical Report', TVA-TR75-1A, Revision 9,

which was; developed to resolve past problems relating to the

inability of management. to take prompt effective corrective

action to. prevent recurrence of problems.

The past problems

were under consideration for escalated enforcement at the start

of the basis period.

During the basis period, Sequoyah began

implementing the.new topical requirements which involved hiring

the additional- staff required,' training them to appropriately

c

implement 1the program, and then monitoring the implementation to

ensure thatithe desired results were achieved.

During this

transition period Sequoyah experienced significant implementa-

tion problems especially with the conditions adverse to quality

'(CAQR) program which was the subject of several TVA audits and

.NRC inspections.

The TVA audits concluded taat the root cause

of the failure.of theLprogram to not fully process any signif-

icant CAQRs'was due to a lack of line management and Quality

Assurance (QA) management involvement and attention.

This was

the same reason the previous corrective action program hadn't

been effective.

Sequoyah responded by deeply involving upper

level managers in the corrective action program implementation.

While . problems still existed in the QA program implementation,

the staff concluded that the program began moving in a positive

direction toward the end of the basis period after upper level

management involvement had significantly increased.

Based on

'

'

the shutdown plant enforcement policy and implementation of an

acceptable corrective action program prior to restart, the past

problems were given' discretionary enforcement.

.

The three ' safety committees which functioned during the basis

f

period [ Plant Operations Review Committee (PORC), Nuclear Safety

Review Board (NSRB), Independent Safety Engineering Group

{

,

(ISEG)] went through a change process due to TS changes and

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f

charter reviews, which were for the most part a result of NRC

initiatives.

PORC was initially ineffective, however, improve-

ment-was observed near the end of the basis. period due to both

the qualified reviewer TS change and a new plant manager.

The

NSRB and ISEG did not independently identify issues which

produced substantive changes to the site.

During the basis period, 88 LERs were issued of which 26 were

classi fied as significant. These resulted primarily from the

design reviews which TVA had initiated.

Some LERs were unclear

with respect to the root cause determination of events or

differed from the staff determinations.

The licensee esta-

blished an ISEG audit, identified similar concerns, and was

implementing ISEG and NRC recommendations at the end of the

basis period.

j

Both the Special Employee Concerns Task Group (ECTG) and the new

!

Employee Concerns Program (ECP) were in existence during the

basis period.

The ECTG was working on resolution of the

concerns which it received in the 1985 to early 1986 time frame.

q

Numerous revisions to the ECTG reports and their corrective

l

actions occurred as a result of NRC review.

All employee

{

concerns received during the basis period were processed through

the ECP.

The NRC identified weaknesses relating to resolution

of generic Lconcerns, administrative issues, and restart

determinations which were.promptly addressed and corrected by

the ECP management.

NRC reviews of both programs indicated that

l

concerns were being adequately addressed at the end of the basis

period.

j

l

TVA Nuclear Power corporate management was usually involved in

Sequoyah site activities in an effective manner during the basis

period. There were several management changes at the site which

contributed to major improvements in operation, security and

radiological controls during this period.

There were corporate

audits made in the radiological controls and maintenance areas

where actions were taken by corporate management to strengthen

these programs.

Although many significant problems in programs

at the site were not being identified by TVA prior to NRC

inspections, usually strong corrective actions from the corporate

'

level were taken when it was needed to correct the identified

problems.

For the basis period, corporate management was generally

responsive to NRC initiatives.

Responses to NRC were generally

timely and generally sound and thorough.

This is shown in the

significant amount of work completed by the staff and TVA in the

basis period.

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The staff conducted an inspection of management effectiveness

1

related to licensing _ activities in the basis period.

The

inspection was conducted in key areas of responsibility at both

the plant site and corporate offices. The staff concluded that

corporate management processes in the areas inspected were

functioning adequately.

B.

Assessment Period Summary (February 4,1988 - February 3,1989)

Sequoyah has been operated in an overall safe manner during the

assessment period.

Management involvement in and attention to the

operations and support of the plant has significantly improved as a

result of the strong leadership exhibited by the new plant a.anager

and new site director.

The plant operations area matured during the assessment period. After

starting the assessment period with five reactor trips, Unit 2 was on

line for 210 continuous days which established a TVA single unit

record.

Unit 1 experienced two reactor trips during startup with

full availability for the rest of the assessment period.

Strengths

included the procedures upgrade programs, the emphasis on procedural

compliance, and the ownership concept for the operators.

Corrective

activs for problems once the root cause was identified were consider-

ed a strength. Weaknesses included operation of the radwaste system;

-

root cause analysis in relation to the post-trip cooldown shutdown

margin issues; and the performance of fire watches.

Control of plant

activities by the control room operators improved during the latter

half of the assessment period.

The overall. quality and experience level of the health physics staff

is _a program strength, and the licensee's health physics, radwaste,

and chemistry staffing levels are adequate and compare well with

other utilities having facilities of similar s,ize.

Management

provides adequate support and is involved in matters related to

radiation protection.

The maintenance / surveillance area also matured during the assessment

period. Strengths included the leadership exhibited by the new main-

tenance superintendent. the establishment of the work control group,

the establishment of a preventive maintenance upgrade program,

implementation of the system and train outage concept for scheduling

maintenance, and implementation of the system of the month review

program.

Weaknesses included the large number of personnel errors or

inadequate procedures which resulted in Engineered Safety Feature or

reactor protection system actuations; the inability to produce

realistic schedules; and the inability to correct problems associated

'

with the feedwater control system.

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During a full' participation exercise, the licensee demonstrated

'

that they could satisfactorily respond to an emergency at the

facility.

However, weaknesses were noted in that the licensee had on

two' occasions failed to promptly report a Notice of Unusual Event

(NOVE) and also failed to recognize an explosion as requiring entry

into the emergency classification logic during the emergency

j

exercise.

In the security area, a high number of hardware equipment inade-

quacies exist.

These inadequacies, which are a result of the

security equipment being obsolete, have lead to a continuous depen-

dence on compensatory measures.

Corporate support was weak because

of a high turnover rate; however, the licensee has finalized a

reorganization of its Corporate Nuclear Security Service Branch which

has resulted in some improvements.

The site management has been

instrumental in dedicating site support to help the security branch

reduce the number of security compensatory measures.

The Engineering / Technical Support ac'tivities did not significantly

i

exceed minimum regulatory requirements.

While numerous issues were

resolved - during the assessment period, many of the issues were

resolved only after considerable NRC input.

Support for operations

I

of the plant was initially viewed as a weakness but improved late in

the assessment period.

4

In .the Safety Assessment / Quality Verification area, the most

~

important improvement was in the corrective action program which made

significant strides during the assessment period.

Strengths included

.

the significant management attention to and involvement in the

corrective action process, the strong leadership provided by the

' j

plant manager and new site director in getting employees to accept

'

responsibility for doing quality work, the quality monitoring and

audit program, and the employee concerns program.

Weaknesses in-

cluded the 10 CFR 50.59 safety evaluation program and the slipping of

the dates and scope changes for commitments made to the NRC.

3

C.

Overview

February 4,1988 - February 3,1989

Functional Area

Rating

Trend

,

Plant Operations....................

2

None

Radiological

Controls...............

2

None

Maintenance / Surveillance............ 2

.None

Emergency Preparedness.............. 2

None

Security............................

2

None

Engineering / Technical Support....... 3

Improving

Safety Assessment /

'

Quality Veri fica ti on. . . . . . . . . . . . . . 2

None

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III. CRITERIA

Licensee performance is assessed in selected functional areas, depending

on whether the facility is in a construction or operational phase.

Functional areas normally represent areas significant to nuclear safety

and the environment.

Some functional areas may not be assessed because of

little or no licensee activities or lack of meaningful observations.

Special areas may be added to highlight significant observations.

The following evaluation criteria were used, as applicable, to assess each

functional area:

1.

Assurance of quality, including management involvement and control;

2.

Approach to the resolution of technical issues from a safety

standpoint;

3.

Responsiveness to NRC initiatives;

4.

Enforcement history;

5.

Operational and construction events (including response to, analyses

of, reporting of, and corrective actions for);

6.

Staffing (including management); and

.

7.

Effectiveness of the training and qualification program.

Nowever, the NRC is not limited to these criteria and others may have been

used where appropriate.

On the basis ~ of the NRC assessment, each functional area evaluated is

rated according to three performance categories.

The definitions of these

performance categories are as follows:

1.

Category 1.

Licensee management attention and involvenient are

readily evident and place emphasis on superior performance of nuclear

,

safety or safeguards activities, with the resulting performance

i

substantially exceeding regulatory requirements.

Licensee resources

are ample and. effectively used so that a high level of plant and

i

personnel performance is being achieved.

Reduced NRC attention may

l

be appropriate.

2.

Category 2.

Licensee management attention to and involvement i r.

the performance of nuclear safety or safeguards activities is good.

The licensee has attained a level of performance above that needed to

,

meet regulatory requirements.

Licensee resources are adequate and

j

reasonably allocated so that good plant and personnel performance is

1

being achieved.

NRC attention may be maintained at normal levels.

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3.

Category 3.

Licensee management attention to and involvement in

the performance of nuclear safety or safeguards activities are not

sufficient.

The licensee's performance does not significantly exceed

that needed to meet minimal regulatory requirements.

Licensee

resources appear to be strained or not effectively used.

NRC atten-

tion should be increased above normal levels.

The SALP Board may also include an appraisal of the performance trend

of a functional area.

This performance trend will only be used when

both a definite ' trend of performance within the evaluation period is

discernable and the Board believes that continuation- of the trend may

result in a change of performance level.

The trend, if used, is defined

as:

Improving: Licensee performance was determined to be improving near

the close of the assessment period.

Declining: Licensee performance was determined to be declining near

the close of the assessment period and the licensee had not taken

meaningful steps to address this pattern.

1

IV.

PERFORMANCE ANALYSIS

A.

Plant Operations

1.

Analysis

.

The quality of operations at Sequoyah improved during the SALP

assessment period based on the results of routine and special

inspections.

During the first half of the assessment period,

several plant -trips and operational events occurred which

demonstrated that the operations area required further improve-

ment.

Following an NRC/TVA management meeting to discuss the

root causes of the poor performance which caused the trips, the

i

Sequoyah plant staff exhibited increased responsiveness to NRC

l

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issues, attention to detail, and commitment to quality.

Increased management attention to and involvement in the opera-

tion of the plant contributed to a Unit 2 record power run

following the management conference.

Management initiatives

included revisions to the root cause assessment procedures,

establishment of a requirement for PORC approval of post trip

reviews prior to restart, increased attention to control of

plant activities, and a conscientious effort to reduce the

number of inoperable or out of service components.

i

Management attention to and involvement in the upgrading of

. operating procedures were focused both by results from NRC

!

inspections, which occurred near the end of the basis period and

,

l

during the assessment period, and by licensee initiatives.

Operating procedures were included in the licensee's ongoing

procedure enhancement program.

Standardizing the procedure

.

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format and clarifying instruction steps as part of the

enhancement program were elements of the program initiated

during the latter part of the assessment period.

This is a

long-term program and is not expected to be complete during the

next SALP rating period.

System Operating Instruction (S01)

checklists were reviewed and revised by the licensee after NRC

inspections during the basis period revealed prcblems with the

system alignment processes.

After the licensee completed these

revisions, system operating instructions were workable and

adequate.

However, the procedure change process was difficult

and cumbersome.

The use of night orders to circumvent the need

to revise operating procedures was stopped.

TS' interpretations

were upgraded and now require specific approval prior to their

entry into the TS Interpretations log.

The Emergency Operating

Procedures (EOPs) were determined to be adequate and the

corrective actions initiated by the licensee from a basis period

inspection were determined to be appropriate.

The

Administrative Instruction for controlling Hold Orders was

revised to require more control by the Operations staff and more

responsibility by the persons performing the work resulting in

an improved hold order process.

Upgrading cf the system logic

drawings for those systems. described by the Design Baseline and

Verification Program (DBVP) boundary was completed during the

assessment period and the drawings were returned to the control

room for use by the operators.

Also, drawings essential for

safe plant operations were available in the control room.

At

the end of the assessment period, a lcrg-term effort was in

progress to restore other system logics to the prinary drawirg

list and return them to the control room.

The licensee's approach to the resolution of technical issues

from an operational safety standpoint was technically sound. An

understanding of the safety aspects was apparent, and censerva-

tism was usually exhibited when responding to scfety-significant

events and issues.

Notable exceptions to this generalization

were the poor planning and management ineffectiveness in dealing

with the system alignment and operability determination in

support of UHI valve repair, and in the resin transfer opera-

tions which occurred near the end of the assessment period.

Several operational plant events that occurred during the

restart of both Units 2 and 1-identified that a poor feedwater

control system design and operating philosophy existed.

Changes

to procedures and specifi'c operator training to eliminate trips

and transients in this area were not initially effective. Rect

cause determinations did not involve sufficient first line

operations management efforts which resulted in a protracted

resolution process.

Improvements in the area of communications were instituted

following an incident involving manipulation of the wrong valve

by an auxiliary unit operator which resulted in a loss of RHR

suction.

Control room professionalism was adequate and showed

_ - _________-_ _

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continued improvement during the assessment period.

The

control

room was upgraded through extensive cosmetic

improvements such as new carpeting, painting, and repair of

deficiencies such as roof leaks.

However, several functional

deficiencies exist which affect operator performance and

effectiveness.

Nuisance alarms, long-sta.nding hold orders and

Temporary Alterations (TACFs), and human factors problems

associated with steam generator level controls continued to

cause an unwarranted number of problems for the operators.

Management was aware of these problems and is addressing them in

the form of a System Engineering concept and a detailed control

room design review.

Problems continued in the configuration control area (system

alignment) through the startup of Unit 2 particularly in the

area of waste water systems.

The program for controlling the

configuration and operations of the waste water systems was

changed to provide the same level of control for these systems

as was. applied to other plant systems that are under the

authority of operations.

This proved to be a positive step in

.,

reducing configuration control errors associated with the waste

water systems.

Additional changes made in the configuration

control program consisted of repeat back communication, and

separating the first and second verification by time and distance.

The latter change had been previously recommended during the

basis period by the licensee's Unit 2 operational readiness

review team, but had not yet been implemented by managcment.

Once implemented, these changes significantly reduced configu-

l

ration control problems.

The licensee performed evaluations to confirm that compensatory

measures which had previously been established for disabled

safety functions were properly documented and were collectively

and individually capable of being performed with normal staffing

levels.

Operator awareness and control of long standing TACFs

in relation to their effect on plant configuration was a matter

of concern to the NRC during the basis period and continued to

be an issue during the assessment period.

The licensee took

action to reduce the number of TACFs to approximately 80, which

was 50% of the level at the beginning of the period, with a goal

of having no more than approximately 30 TACFs.

Operators were well informed in the use of emergency operating

procedures.

Because of the long duration shutdown period

(approximately 21 years), the number of reactor operators

experienced in power operations was low and additional support

personnel were made available in preparation for Unit 2 restart.

These included additional management presence in the control

room, additional control room Senior Reactor Operators, and

temporary Operating Shift Advisors.

Operator actions for most

events that occurred during the Unit 2 startup were appropriate.

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Licensed operators responded effectively to plant transients on

most occasions during Unit 1 startup

including a reactor trip

of Unit'l caused by' feedwater control problems, a turbine trip

of Unit 1, a reactor trip of Unit 1 caused by a generator

ground, and a lightning strike of a switchyard transfonner

during a thunderstorm.

.

Operators were observed to be disciplined professionals with

adequate communication skills.

However, occasional lapses which

were exemplified by one instance of inadequate action by an

operator during routine plant activities occurred.

This example

involved the placement of a centrifugal charging pump in the

pull to lock position which resulted in a failure to comply with a

technical specification action statement,

Control room activities were generally conducted in an effective

and professional manner.

Formal communications were observed in

most cases.

Operators were attentive, aware of plant conditions

and responsive to changes in plant conditions.

Senior plant

management actively supported the above operator activities and

i

was deeply involved in the day-to-day operation of the plant.

In addition senior plant management maintained a detailed

account

of

and

tracked

the status of known equipment

deficiencies, CAQRs, and plant parameters in daily plant

meetings.

Active involvement by plant management and support of

ti.e ownership concept by the operations department had a

-

positive' effect on plant operations and morale.

This was

exhibited by the absence of significant- events or operating

problems during the extended power run of Unit 2.

Facility

operations reflected improvements in planning and assignment of

priorities during the period.

The forced outage rate for both

units during the period was extremely high as a result of the

extended shutdown.

However, following the five Unit 2 trips

which occurred early in the Unit 2 startup process, Unit 2 had

no forced outages for a period of approximately 210 days.

Unit 1 experienced two reactor trips during its startup period,

followed by full availability for the remainder of the

assessment period.

Management support and insistence on the ownership concept has

strengthened the authority and role of the Operations group in

general and the control room shift supervisor in particular.

Operations personnel have demonstrated on many occasions their

willingness to suspend or delay surveillance, maintenance ard

other schedule impacting activities until they were satisfied

that the plant was in a safe stable condition and that other

plant activities in progress would not interact with the

scheduled activities to produce safety system actuations. The

absolute authority of the operations staff in these matters has

been fully supported by plant management.

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24

During the assessment period the licensee administered

i

requalification examinations.

The results from the examinations

indicated a large percentage success rate (approximately 69 cut

of 70).

Nonlicensed operators were judged to be extensively

trained receiving both detailed classroom training and thorough

{

in plant on the job training.

The percentage success rate for

"

new operating license candidates was determined to be

below average (7 out of 11 passed).

Operations shift training for newly installed plant modifica-

,

tions and for correction of operating deficiencies or events was

i

adequate.- However, occasional lapses were exemplif.ied by the

shutdown margin / excessive cooldown events and rod control demand

counter problems.

During the assessment period Operating shift manning was

l

adequate and maintained at the levels established during the

basis period.

Several management positions were eliminated to

streamline the Operations organization which resulted in a more

effective organization.

Management stressed procedural compliance by operations per-

sonnel throughout the assessment period.

This had a side effect

of improving procedures by forcing operators to have inadequate

procedures revised before they could be used.

However,

instances of procedural non-compliance and deviation continued

during Unit 2 startup, such as the MSIV closures, configuration

control deviations, and Upper Head Injection (UHI) accumu'lator

venting events.

Management was very aggressive in responding to

the above issues and by the middle of the assessment period

procedural adherence was adequate and improving.

In an event involving the discharge of highly-radioactive spent

resin that occurred during the lctter portion of the SALP

assessment period, it was determined that the intense management

attention given to power operations had not been applied to the

waste processing portion of the power plant and the attendant

operations support staff.

This event highlighted, in that area

alerte, inadequate procedures, a casual attitude toward following

procedures, inadequate drawing control, and failure to aggres-

sively correct design problems that make cperations awkward or

could create personnel or radiological hazards. In addition,

plant management in this specific area appeared to be

poorly

trained and very weak with respect to the operating and physical

characteristics of their assigned system.

Finally, interactions

between the waste and water management group and other plant

management that were observed following this event did not

demonstrate a cooperative, quality-oriented approach to the

resolution of technical issues within the waste and water

management group.

Plant management is currently taking strong

corrective action to improve the waste water processing area.

_-

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L

Logkeeping by licensed operators continued to exhibit weaknesses

particularly -in the areas of detailed entries, entry and exit

from Limiting Condition for Operation (LCOs), and descriptive

explanations and rationales for decisions made and actions

conducted by the operators and SR0s.

During the last' two moriths-

l

of the assessment period, Operations management implemented

'

corrective actions in these areas by having' Operations super-

visors review logs for completeness, stand-alone entries and

supportable explanations for LC0 entries, exits and changes to

plant and equipment status.

The NRC identified during the

latter portion of the assessment period a significant

improvement in the level of detail supporting log entries.

The

corrective actions were effective.

Operational events in general were promptly and accurately

identified.

Exceptions were the failure of the operations staff

'

to recognize problems with the excessive post-trip cooldowns,

and having a centrifugal charging pump in pull-to-lock while the

other pump was inoperable, both of which resulted in escalated

enforcement.

Emergency Notification System (ENS) reports occurred at a high

rate as a result of the special outage conditions and system

configurations.

Notifications were generally conservatively

made 'and technically correct.

ENS notification was not made

initi, ally for the centrifugal charging purp in pull-to-lock

-

event,. and for an unidentified RCS leakage above allowable

incident.

DNE support of Operations in making Operability

'

determinations improved during the assessn.ent period.

This

improvement was the result of management initiatives and

personnel changes.

As a result of the change in licensee management that occurred

at the'end of the basis period, PORC reviews became aggressive

and technically involved in the resolution of issues affecting

the safe operation of the unit.

Changes in PORC activities

which resulted in improved performance included consistency in

personnel staffing and the high expectations established by the

new plant manager.

The elevated expectations were also strongly

supported by the new site director and upper TVA management. As

a result of the TVA management initiatives, the Plant Operations

Review Staff was established as a part time support group for

PORC.

P0RS employed specialized training and skills to perform

root cause evaluations and determine corrective action plans

associated with plant events, which were then submitted cs

completed projects to PORC.

The use of the Plant Operations

Review Staff has involved the PORC deeply in day-to-day plant

operations.

i

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w[

eat the close of the:SALP assessment period Sequoyah upper line

'

~

management was found to .be strongly comnitted to obtaining

"

quality'in plant operations. .There was also a general increase-

.

.in management attention toward the ccnduct of operations and-

l

. management awareness of plant conditions.

These, coupled with

!

organizational changes to reduce both. management resistance to

i

change; and the number of management levels, resulted in _ _

l

continuing improvement'in the performance of the operating staff

l

'

-

and the resolution of technically diverse and complex issues

!

$

throughout the year.

p

i,

During this assessment period the entire fire protection staff

at Sequoyah was reorganized into a Fire Operaticns Unit.

The

l

Fire Operations Unit consists of a dedicated fire brigade which

'is responsible for fire suppression and fire prevention

,

inactivities.

The dedicated fire brigade replaced the preexisting

]

system of_ a fire brigede composed of unit operations personnel.

1

Fire: brigade' training at TVA's Nickajack Fire Training Center

j

was fourd to be excellent and brigade manning was determined to

i

be adequate.

Reorganization of the fire protection staff

j

. greatly improved fire brigade effectiveness and fire prevention

!

activities during this assessment period. Organizational

i

planning and assignment of- priorities was demonstrated in the

l

fire ' brigade reorganization.

In general, policies and pro-

,

cedures were well stated and understood.

~Under the reorganized

!

'

fire operations unit, decision making was usually at a level

!

that ensured adequate management review.

Involvement by

"

corporate management in the fire protection area was evident.

Two . Fire' Protection QA Audits were performed during the SALP

j

i

'

assessment period, one of which was by the licensee's insurer,

. American , Nuclear Insurers ( ANI).

These audits icentified a

i

number of unsatisfactory conditions and findings and reccarended

i

several program improvements.

The licensee either implemented

i

E

the - corrective actions associated with these findings or

evaluatcd the issues to develop a schedule date for completion

of the corrective' actions.

The NRC identified weaknesses

in

~

the areas of procedural implementation of fire penetration

,

barrier requirements and control of combustibles. The new fire

i

protection management was aggressive in the resolution of these

i

issues and appeared to take appropriate corrective actions.

!

!

. The condition of Fire 4arriers, surveillance of fire protection

l

^

syst' ems and components, emergency lighting, manual equipment and

l

QA audits were satisfactory in terms of the low number of

l

deficiencies noted.

Housekeeping practices and conditions

relative to fire. protection wera found to be adequate.

l

l

During the SALP assessment period inadequacies in the perfor-

mance of fire watches were noted.

The inadequacies consisted of

inadequate inanagement oversight in regar d to fire watch per-

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27

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sonnel and failure. of management to provide concise guidance on

how fire watch individuals must perform their duties.

This

issue occurred at the time that the new organization was being

put into place and was aggressively pursued by the new fire

organization management.

Five violations and one deviation were identified:

j

a.

Severity Level III violation for failure to comply with TS

!

3.0.3 involving loss of safety functions and for failure to

notify the NRC in a timely manner. (88-20-03 & 88-20-04)

b.

Severity Level IV violation for failure to implement

configuration controls. (88-26-01)

c.

Severity Level IV violation for failure to meet require-

ments of TS 3.3.1 and 3.3.2 to place OTDT and OPDT in trip.

(88-39-02)

d.-

Severity Level IV violation for failure to perform fire

watch patrols.

(88-46-01)

e.

Severity Level IV violation for performing a test of the

TDAFW pump without a written procedure.

(88-48-02)

f.

Deviation for failure to comply with a commitment made

concerning the control of combustibles (wood) in safety-

related areas.

(88-54-01)

.

2.

Performance Rating:

Category 2

3.

Recommendations:

The Board recognized that significant experience was gained

through the plant events and activities which occur ed

,

during the assessment period and resulted in an improvement

in the plant operations area.

!

B.

Radiological Controls

1.

Analysis

During the assessment period, inspections were performed by the

resident and Regional office staff in the areas of ram *+'on

protection, radiologi, cal effluent, and confirmatory meure-

ments.

Included in the inspection program was a special team

inspection for restart of Unit 1 and a special team inspection

to assess the performance of health physics, chemistry, and

radioactive waste processing during the recent outage.

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The' qualifications of the new Superintendent of Radiological

Controls posi* ion were determined to have met the requirements

- discussed _ in Regulatory Guide 1.8, Qualification and Training of-

Personnel for Nuclear Power Plants.

The licensee's health physics, radwaste,. and chemistry staffing

levels were adequate and compared well with other utilities -

having' facilities of'similar size.

An adequate number of ANSI

qualified licensee health physics (HP) technicians were

available to support . routine operations.

During outage

operations, additional contract health physics technicians were

used to supplement the permanent health physics staff.

The

overall quality and experience level of the health physics staff

is-viewed as a program strength.

Radiation protection training

was considered good.

The licensee's general employee training

(GET) in radiation protection was well' defined.

The GET

training / retraining program not only included standard topics as

outlined in 10 CFR 19, but findings of licensee audits and NRC

inspections were factored into the training.

Management support

of and commitment to training was evident in that sufficient-

time was allowed for training and employees were encouraged to

attend.

Management support and involvement in matters related to

radiation protection were demonstrated by:

(1) purchasing an

automated laundry monitor to control the potential for " hot

-

particles" in order to reduce exposure to personnel;

(2) installir.g seven sensitive portal monitors at the exit to

the . radiation controlled area (RCA) to be more effective in

detecting personnel contaminations; (3) establishing an ALARA

incentive program; and (4) providing corporate support in

resolving technical isst'es as related to the radiation protec-

-tion program.

Resolution of technica: issues was generally adequate; however,

a special team inspection observed, during the Unit 2 refueling

outage at the end of the assessment period, that the licensee

experienced problems in containment such as high iodine airborne

radioactivity, an unexpected increase of beta radiation levels in

steam generators, and heat stress to personnel while wearing

supplieu oar noods.

These problems appeared to be caused by a

failure of licensee management to communicate and evaluate these

problems adequately.

Early identification and technical resolu-

tion of the root causes were not performed in a timely manner,

which created the need for increased radiological attention,

resources, and demand for support from the radiological controls

program.

During the assessment period, a special NRC inspection team

revievied the licensee's controls for high radiation areas and

determined tw tnese controls were generally adequate.

l

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i

However, one violation was identified pertaining to two

-

. Assistant Unit Operators (AU0s) who were unknowingly working in

I

-a high. radiation area in the Unit 1 Auxiliary 8uilding created

l

by an inadvertent introduction of-reactor coolant and resin into

j

the CVCS demineralized resin transfer piping. The AU0s received

!

l

doses of between 400 and 500 mrem and did 'not exceed .any

administrative or NRC exposure limits. . It was determined that

~ the area was posted as a radiation area 'instead of 'a high

l

radiation area 'and that the workers had neither an integrating

l

dose . rate monitoring device nor an individual present with a

dose rate' monitoring device to provide radiological protection

job coverage. The licensee's immediate corrective action was to

post and lock the concerned high radiation area and to reconfirm

i

that other radiation and high radiation areas were adequatelv

controlled.

i

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'

~The

respiratory protection

program was

reviewed by

the NRC during the assessment period and it was determined to t

the program was well defined and implemented in accordance with

appropriate regulations.

The 1987 collective radiation dose was 206 person-rem which was

I

'

approximately 56% of the national average of 368 person-rem pe'r

pressurized water reactor (PWR).

In 1988, the - station's

collective radiation dose was 382 person-rem, compared to 345

person-rem per unit national average, which when combined with

1

the 1986 and ~ 1987 collective radiation dose ' averaged 284

person-rem for three years.

However, since the unit has been

inoperative for an extended period

the three ~ year average is

not necessarily comparable to similar intervals for other units.

At the end of 1987, the area of the plant controlled as

radioactively

contaminated was approximately 15% of the total

area which potentially cruld become contaminated. At the end of

1988, the area contaminated was still approximately 15% and

slightly above other facilities similar in design, however, this

did not create a significant personnel exposure or personnel

contamination problem.

The licensee experienced 130 personnel contaminations in 1987.

The number of personnel contaminations in 1987 was among the

lowest in Region II.

However, in 1988, the number of personnel

l

contaminations increased to 409 and 155 of these were skin

l'

contaminations.

The increase in personnel contaminations was

due in part to startup activity at the plant, increasing

radiation levels and the increased detection sensitivity of the

new, more sensitive, portal monitors at the exit of the RCA.

Effluent summary data for 1985, IS86, and 1987, are contained

under Supporting Data and Summaries,Section I of this report.

These releases are consistent with the plant being shut down

from mid-1985_through 1987, and consequently no basis exists to

establish any trends during the assessment period.

_

_ _ _ _ _ _ _ _--___-_ _ ____ _ _ _ -

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30

~

During the' assessment period, the licensee's program for

l'

packaging, shipping, and storage of icw level radioactive waste

was - determined to be adequate.

The licensee demonstrated good

w

radioanalytical trend capability by' showing close agreement with

NRC results for both beta-emitting and gamma-emitting samples.

However, weaknesses were identified in the radiological waste

'

. water processing area as described in the operations section.of

this assessment.

g

Two violations were identified:

a.

'Ssverity. Level IV violation for failure to adhere to or '

-

establish' procedures for performing breathing: zcne air

samples and for exposure control during steam generator

work.

(08-31-02)

b.

Severity Level IV violation for failure to evaluate

the radiation hazards present in the 690 foot eleva-

tion Pipe Chase in the Auxiliary Buildine.

(89-05-04)

2..

Performance Rating:

Category 2

3.

Recommendations:

.

' Hone

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C.

Maintenance / Surveillance

.1.

Analysis

During the assessment period, the technical quality of main-

tenance and surveillance at Sequoyah was good as a result of the

many technical and programmatic upgrades which occurred.

These

l

programs experienced substantial organizational and~ perscnnel

changes resulting in a large number of licensee initiatives.

The addition of a new maintenance superintendent at the

beginning of the assessment period . resulted in licensee

initiatives in the maintenance area which included; increasing

the use of system engineers, the use of.new vibration monitoring

equipment techniques, maintenance procedure enhancement,

extensive Motor Operated Valve Actuators (M0 VATS) testing of

primary and balance-of-plant valves, establishment of a 24 hour2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br />

Outage Manager to coordinate maintenance and triodification work,

and the organization of maintenance and modification activities

l

into train and system outages.

Management of the Maintenance

Program was very effective as demonstrated by positive trends in

industry indicatcrs such as maintenance backlog, tagging,

overtime use, CAQR and LER generation, QA document rejection,

Post Modification Testing (PMT) rejection requiring maintenance

_ _ _ _ _ _ _ _ - _ _ _ - _ _ _

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31

~

rework, personnel contamination, industrial safety practices,

and delinquent safety-related preventive maintenance.

Line

management increased its presence in the operating and work

spaces, became more aware of plant status and technical issues

and demonstrated a. commitment to the program and associated

improvements implemented during the assessment period.

The licensee developed a detailed program for completed

l

L

maintenance record review, which is quite thorough and effective

l

in identifying and correcting deficiencies.

The use of

procedures in accomplishing maintenance activities was adequate

and improving. The quality of procedures and work requests, and

their associated review, steadily increased as a result of

Maintenance Section upper and middle level management

involvement in the licensee's program for removal, repair and

restoration of safety-related equipment. The licensee initiated

a system / train outage concept which was coordinated with unique

site electrical distribution and TS requirements.

In addition,

the licensee instituted a standard maintenance practice which

established the niethod for managing, tracking, planning,

scheduling, post work evaluation of and documentation of main-

tenance work activities.

This establishment of administrative

control over maintenance work activities reduced open-ended

" Troubleshoot and Repair" type work orders and provided clearer

direction to the personnel performing work in the field.

Operability determination was also added to the administrative

control process prior to closing out work orders.

The licensee's action with regard to NRC maintenance related

initiatives was generally good.

The response varied depending

on the organizations involved and the time during the assess-

ment peciod when the NRC initiatives occurred.

Licensee

response improved in all areas throughout the assessment

period.

Responses from onsite maintenance and modifications

organizations were usually quick, professional and technically

accurate.

During the initial portion of the SALP assessment

period, support for onsite maintenance related issues from the

TVA DNE organization took long periods of time.

This caused

issue resolution and operability determination to lag.

However, by the middle of the assessment period DNE support

for maintenance and modification activities was much improved.

Licensee resolution of maintenance related technical issues

usually indicated technical understanding of the issues,

operational conservatism, and was generally well thought out.

Examples of well thought out maintenance activities were;

RCP trip bus troubleshooting and repair, and steam generator

tube leak resolution and preventive plugging.

Those main-

tenance activities that were less professionally addressed

by the licensee included pressurizer safety valve trip

setpoint calibrations which occurred at the beginning of

the assessment period.

_ _ - - _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ - - - _ - _ - _ _ - _ _ _ _ _ - _ _ - _ _ _

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The maintenance staff is generally well qualified and trained.

Special training was given to maintenance personnel following

4

issues related to the maintenance management system, EQ, conduct

{

of testing, and configuration control.

Trrining also included

j

management training for all levels of liaintenance Department

i

management and specific technical training for first and second

line managers to increase in-craft and cross-craft supervisory

expertise.

The experience levels of maintenance department

first line supervisors averaged approximately 10 years of craft

related experience, which included several hundred hours of

craft and engineering training.

The site maintained the INPO

training accreditation reccived during the basii period for

maintenance training.

During the assessment period, outage and work control

processes were established and implemented.

Performance

immediately improved due to planning and assignment of

priorities.

Procedures for control of these processes were well

defined, and appeared to be understood by the personnel involved

in their implementation.

The technical background and level of

plant systems knowledge of the planners, coordinators and

managers in the work control / outage organization was excellent.

These positions were filled with operators, engineers, and

managers that were deeply involved in the day-to-day operations

of the plant and demonstrated excellent communications and

organizational skills.

'

While maintenance tracking and planning was considered a

'

strength, maintenance outage stheduling was considered to be a

weakness.

The licensee demonstrated it was capable of drafting

detailed correct 1<e and diagnostic niaintenance plans, and

1

implementing those plans in the field.

However, outage and

maintenance schedules rarely had any realistic relation to the

actual work being performed in the plant and exhibited continual

and predictable schedule slips.

The licensee used the composite maintenance crew concept for

NOVATS testing, refrigeration, and general maintenance. An NRC

review of the implementation of the composite crew process at

the begining of the assessement period revealed that no

procedures addressed the training and qualifications require-

j

ments for foremen supervising personnel in other crafts, for

'

craftsmen performing work outside of their craft, or for

craftsmen performing independent verification outside of their

craft.

Although no plant events were attributable to composite

crews during the assessment period, composite maintenance crews

existed in, contradiction to the training and qualification

requirements for maintenance foremen and craftsmen. This

indicated insufficient management attention to and involvement

with the composite crew concept and represented a failure by

management to recognize that minimum regulatory requirements

_ _ _ _ _ _

_ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _

_ . _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ . _ . _ _ _ _ _ _ _ _ _ _ _ _ _ _

,

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33

were not being met. Once management attention was focused on-the

~

problem, a comprehensive procedure was developed to address the

composite maintenance crew concept.

Corrective actions that

were initiated appeared to have resolved problems with the

composite crew concept.

The. control and use of calibrated equipment met regulatory

requirements and purchase receipt inspection and traceability of

installed materials was found to be acceptable.

Additionally,

Lpost maintenance testing was found to be satisfactorily

accomplished.

During the assessment period the material condition of

. plant components steadily improved. A review of system failures

did not indicate any adverse management or maintenance

practices.

Several conditions that did not constitute failures

but did affect plant operations were: leaking pressurizer safety

valves on both units, a leaking reactor vessel flange 0-ring on-

Unit 1, and unstable feedwater automatic controls for both

units.

In the case of the Unit 1 pressurizer safeties and the

Unit 1 vessel flange ~ 0-ring, plant activities were well

controlled and personnel involved were technically astute and

receptive to NRC initiatives.

However, in reference to

feedwater controls, less than cohesive disciplined management

activities were'noted.

The plant's material condition, preservation, and housekeeping

.

status was adequate. Occasionally maintenance debris and other

material / housekeeping deficiencies existed in the auxiliary

L bu11 ding and other plant spaces.

Additionally, work in progress

was often left open, uncovered, and unattended during work crew

breaks and turnover periods, Examples of these ccnditions were;

ice condenser cleanliness prior to Unit 2 initial heatup, loose

items and debris found by the NRC in safety-related electrical

panels and distribution boards.

During the assessment period the Preventive Maintenance

'

(PM) program at Sequoyah was in the midst of a significant

amount of change.

The licensee initiated a PM Upgrade Program

which was very detailed and resulted in a significant increase

in' the number of PMs required for plant equipment.

This PM

upgrade effort was in place for the majority of the assess-

ment period and the developmental stage will last another year.

Weaknesses were identified in the number of outstanding

delinquent PMs, and the existence of a significant percentage of

recently developed PMs that had never actually been performed on

plant equipment.

The everall conclusion in the Pti area was that

-

a very strong PM program was being developed with involved

management support. The program is being developed as a quality

activity and will improve the safety and reliability of plant

equipment when it is fully impleme 'ed.

The results of this

effort, in the form of benefit to

tant equipment, has r.ot yet

been realized.

.

i

-_ - -_

__

.

I

-

-

..

-

L V

34'

,

Predictive- analysis techniques were well integrated into the

licensee's maintenance program.

Vibration analysis and M0 VATS

testing .were active at the site and were found to be

instrumental- in the. identification of much of the corrective

maintenance.

These two techniques were also found to be used as

an integral part of the licensee's post-maintenance surveillance

activities.

In addition, the licensee implemented a- system

performance monitoring program to improve station reliability.

The program includes vibration monitoring, system and component

. parameter trending, System of the Month reviews, and performance

walkdowns.

Upper plant management is very attuned to the

results from these maintenance techniques and plant operational

decisions were made using this data.

At the beginning of the assessment period, ' management

continued to experience' a lack of . full understanding of the

technical requirements necessary to fully resolve some NRC

identified procurement issues.

Following NRC identified adjust-

ments to the program, Sequoyah established an acceptable program

for resolving replacement part issues.

Following the NRC

findings, management demonstrated a clear understanding of the

issues involved, proposed timely resolution of the findings, and

proposed resolutions which were . technically sound.-

In a

I

specific case (e.g., molded case circuit breakers), Sequoyah

exceeded the. bulletin response requirements which enabled the

NRC to provide up-to-date. guidance ' to other licensees.

In

addition, procurement and maintenance management coordinated

closely during the second half of the assessment period to

,

reduce, by approximately 50 percent, the outage work that could

not be performed due to outstanding material items.

Safety-related equipment storage continued to be well managed

,

throughout the assessment period.

Several cases existed

where detailed storage and material information was necessary to

support plant operability determinations.

In each case the

information was retrieved, clearly' supported operability and

demonstrated a service related role for the storage and

procurement organizations.

Staffing in the procurement and storage areas was adequate.

Staffing of the contract engineering group (CEG) was generally

good. While site and corporate management had the expertise for

the procurement operation, potential impacts on continued

performance were identified as a result of their possible

involvement in other TVA' site procurement activities.

I

During this assessment period, Sequoyah transitioned from a

separate dedicated EQ organization to a matrix organization

within the site DNE organization. This transition occured without

interruption or degradation of the quality of EQ corrective and

l

l:

-

_ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ - _ - _ _ _ - _ _ _ - _ _ _ _ _ - _ _ - _ _ _ _ _ _ _ _ _ - _ _

._

_

.

.

1

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35

preventive maintenance implementation.

EQ maintenance decisions

were made at appropriate levels.

Additionally, plant

organizations had well stated policies to guide them in

completing

field

work.

Management

authority

and

responsibilities were defined and understood in the EQ area.

Sequoyah management continued their resolution of technical

issues in the maintenance area with conservative approaches

during the assessment period.

This was illustrated by the

implementation of corrective maintenance activities to support

the qualification of silicone rubber electric cable installed

inside containment and the qualification of transmitter cable

nylon butt splices.

The maintenance department was adequately

staffed with personnel having the appropriate expertise.

Surveillance performance and technical adequacy continued to

improve through an extensive surveillance review and inplant

validation process that continued throughout the assessment

period.

Surveillance scheduling was reorganized resulting in

only one administrative 1y late TS required surveillance

occurring following the restart of Unit 1.

This improvement in

surveillance management was the result of the licensee's

aggressive SI planning and scheduling program.

The licensee's

scheduling performance of non-TS required surveillance

and

preventive maintenance is less aggressive and appears to rely

heavily on input from upper plant management rather than first

and second line supervision.

In the vast majority of surveillcoces performed implementation

of the surveillance testing was excellent reflecting adequate

planning and assignment of priorities, and indicating an

aggressive level of management overview.

However, surveillance

procedural adherence problems continued throughout the assess-

ment period, although improvement in this area was noted

I

following the initial Unit 2 restart activities.

Exampl'es of

procedural adherence problems were; surveillance of a Reactor

Coolant System (RCS) flow indicator resulting in a reactor trip

when the instrument was returned to service, and a power operated

relief valve (PORV) opening when an RCS resistance teniperature

device (RTD) was returned to service.

Licensee resolution of

surveillance related technical issues reflected a thorough

understanding of the appropriate issues.

Management was

responsive to NRC initiatives in that they established new

surveillance instructions in response to NRC information notices

I

and bulletins.

Personnel performing as test directors while

conducting surveillance testing activities appeared to have a

good working knowledge of the surveilltrce procedures and were

trained in the use of required instrumentation.

_ _ _ - _ - - _ - _ _

__

%

.

36

'

A management initiative, designed to minimize the recurrence of

mispositioned valves, was to form a dedicated Operations

Department surveillance instruction performance team.

Forming

such a team limited the number of people performing surveillance

instructions, increased the exposure of each team member to the

various instructions, and enhanced internal communications.

The

team appeared to be effective in improving efficiency and

control.

The SI team concept was a case of effective technical

resolution and management involvement that occurred during the

assessment period.

,

During the assessment period physics-related activities

associated with the restart of Units 1 and 2 demonstrated the

ability of the licensee to perform at a technical level above

that required to meet regulatory requirements.

A number of

complications were experienced during startup testing, including

significant differences between the measured and predicted

critical boron concentrations on both units and a positive zero

power moderator coefficient on Unit 1.

Licensee management

responded effectively to the complications which were

encountered.

Management ensured that' adequate personnel

resources were allocated to properly perform the test program

and that an atmosphere existed which encouraged feedback from

the ~ersonnel invohed with the testing.

This resulted in a

continuing improvement of the reactor physics testing program.

A significant investment was made in the training of 'inexperi-

-

enced personnel and in the cross training of design specialists,

which should benefit future reactor engineering activities

and result in further improvement of the program.

Marked

improvement in the control of nuclear design calculations

and computer codes was observed during the assessment period.

Management involvement in assuring quality was demonstrated in

that the chemistry program was very actively supported by the

corporate chemistry staff. The staff was involved in developing

a corporate policy statement and directive which established

philosophy, directives and responsibilities for a chemistry

program which endorsed the guidelines recommended by the steam

generators owners group (SG0G) and Electric Power Research

Institute (EPRI).

Management emphasized the need for quality

control in all aspects of the chemistry program to meet the

stringent criteria recommended by SG0G and EPRI for prevention

of corrosion.

Adequate resolution of technical issues was exhibited in the

,,

short term wet layup of Unit 2, the long term dry layup of

Unit 3 and the startup of Unit 2.

Modifications to the moisture

separator reheaters replaced copper-nickel tubes with stainless

steel tubes, reducing the potential sour.ce of copper corrosion

prcducts to the steam generators.

Replacement of all resins in

the polisher vessels prior to restart of Unit 2 was a

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_ _ _ _ _ _ _ _ _ _ _ _ _ _ _

_

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37

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.

'

contributing factor to the good water quality during restart.

Consequently, a lengthy chemistry hold was not necessary.

.

However, the shortage of demineralized water limits the nunber

of polishers that can be used.

The ' licensee has initiated

investigatory programs to improve the all volatile treatment

-(AVT) chemistry control program.

The areas of wet and dry layup

of plant systems, and corrosion and erosion progrems were

determined to be acceptable.

Even though there were major changes in key staffing positions

in the plant water chemistry program, the defined program was

implemented with an adequate number of qualified, experienced

supervisors in accordance with licensee procedures.

As determined at the end of the assessment period, the ISI

program and procedures were acceptable and management

involvement in the ISI process was apparent.

Based on a review

of ISI program submittals and program changes, TVA's responsive-

ness to NRC initiatives and staffing for ISI work was adequate.

During the assessment period the Inserv'ce Test (IST)

program and records were greatly improved and preclude the

problems identified during the basis period.

Management

appeared to be involved in assuring quality in IST activities.

Responsiveness to NRC initiatives was evident.

Based on

observation of in-process testing and review of IST activities,

staffing levels appeared to be adequate.

IST personnel observed

and interviewed in the field conducted themselves in a

professional manner, and appeared to bc well traircd and

qualified for their responsibilities.

Seventeen violations were identified:

a.

Severity Level IV violation for failure to have a procedure

for composite maintenance crews.

(87-78-02)

b.

Severity Level IV violation for failure to adequately

l

implement surveillance

involving RCS temperature,

containment spray system flow, and ice condenser

operability.

(88-02-01)

c.

Severity Level IV violation for failure to adequately

implement work instructions involving resistance

temperature detectors, a system hold onder, and the

safety-related air system.

(88-17-01)

d.

Severity Level IV violation for failure to have an adequate

fire protection surveillance instruction for containment

penetration sleeves.

(88-19-01)

e.

Severity Level IV violation for failure to have an adequate

,

SI for fire barriers.

(88-19-03)

)

f.

Severity Level IV violation for failure to establish and

implement plant instructions (TS interpretations) that

complied with TS 3.7.1.2.

(88-20-01)

E_-----_-----_--.-_---------_----------------__----____--__

_ - - - _ - - _ _ _ - . - - _ - - - - - - - - - - - - - - - - - - - - -

- - _ . - - - - - _ - - - - - - - - - - - - - - - -

--_-------. _ - _

..

-_

---

_

- . _ - _ _

_-

_

.-.

. - . _

, . _ - _ - _ - _

I-

]

...

,

..

. l- ( i

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38

i

a

g.

l Severity. Level IV ' violation for failure to implement

~

,

surveillance requirement 4.5.1.1.1.6 involving cold leg'

j

accumulator boron concentration.

(88-20-02).

1

h.

' Severity Level IV violation for failure to control

maintenance activities related to a steam gen:.-ator level

~

. indicator, and flow transmitter 2-FT-68-718 (88-28-01).

i.

Severity Level IV violation for structural walkdown issues.

-(88-29-02)

j.

Severity Level V violation for failure to control work

practices involving' the installation of beveled washers,

y

spring cans and anchor bolt alignment. (88-29-03)

-l

k.

. Severity Level IV violation for failure to perform an.

adequate ASME section XI test. (88-29-04)

1.

Severity Level IV violation for UHI system inoperable due

.to failure to perform surveillance. (88-34-02)

m.

Severity Level IV violation for EDG surveillance. not

performed when one EDG was made inoperable. (88-34-03)

n.

Severity Level IV violation for two examples of failure to '

follow procedures for radiation monitor work. (88-39-01)'

o.

-Severity Level IV violation for failure to have an adequate

work plan. (88-39-03)

p.

Severity Level IV violation for failure to follow AI-47

requirements. (88-40-01)

'

q.

- Severity Level IV violation for failere to follow incore

flux detector withdrawal procedures. (88-44-02)

2.

Performance Rating:

,.

Category 2

3.

Recommendations:

The Board recognized that improvements in the maintenance area

were the direct result of initiatives instituted by the new

maintenance management.

The Board also recognizes that an

aggressive FM program has been developed, but is not fully

implemented, ind that benefit to the equipment has not yet been

-

.

realized.

.

-

I

,

_-__ _ __ _ __ _ -

r

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39

D.

Emergency Preparedness

1.

Analysis

The inspections conducted curing this assessment period ir.cluded

,

i

two routine Emergency Preparedness (EP) inspections and a full

participation EP exercise.

.

The routine EP inspection performed March 7-11, 1988, disclosed

that the licensee had revised its system for reviewing and

approving changes to the Radiological Emergency Plan and

Implementing Procedures.

The inspection noted that the changes

made under the new system were being properly cpproved and

distributed in a timely manner.

Emergency supplies and

equipment met regulatory requirements.

Although several key

personnel changes had occurred, personnel had been properly

trained prior to integration into the emergency response

organization with one exception.

The exception resulted in a

violation for failure to provide annual retraining to an

alternate Technical Support Center communicator.

In the EP

area, preparedness audits were found to meet regulatory require-

ments.

The routine EP inspection performed Septernber 1-4,

1988,

discicsed that the licensee hcd declared six Notification of

Unusual Events (!!OUE) since February 4,1988.

All events were

promptly classified with the exception of a " seismic alarn

received" on February 8,

1988.

The licensee's failure to

promptly report this event as an NOUE was identified as a

violation for failure to adequately -implement an emergency

procedure.

In addition, a second example of failure to prcmptly

declare an NOUE en high RCS leak rate wcs also identified.

The

licensee was maintaining an adequate notifications and commun-

ications capability in the event of an emergency.

The areas of

shift staffing and augmentation, training, and dose calculation

and assessment were found to be adequate ~.

<

The emergency exercise with full participation was conducte.d on

December 14, 1988, and demonstrated that the licensee could

satisfactorily respond to an emergency at the facility.

The

most significant of the negative observations was a failure of

the Shift Operating Supervisor to recognize an explosion as an

entry into the emergency classification logic.

However, the

licensec adequately demonstrated the ability to classify higher

levels of emergency after entering the emergency classification

logic.

The overall performance was fully satisfactory and an

adequate critique was conducted by the licensee,

i

__-_-__-_______-_____.____-_______-___a

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40

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Three violations were identified.

a.

Severity Level V violation for failure to provide annual

retraining to an alternate Technical Support Center

connunicator. (88-18-01)

b.

Severity Level IV violation for failure to promptly report

an NOUE when a seismic alarm was received. (88-33-01)

c.

Severity Level IV violation for late reporting of a NOUT on

high RCS leak rate. (88-34-04)

2.

Performance Rating

Categury 2

3.

Recommendations

None

E.

Security

1.

Analysis

-

During the assessment period three routine security inspec-

'

tions and one special inspection resulted in the issuance of

three licensee-identified-violations relative to key control,

unescorted visitors and officers being found inattentive to

duty.

The reactive inspection reviewed the licensee's invest-

igation of suspected or alleged drug cbuse and found the

licensee's investigation and resolution to be adequate

In February 1988, the licensee performed both an Operational

Readiness Review (NSB/CA 88-01) and its annual Quality Assurance

Audit (SSA-88-06) which resulted in the identification of

persistent hardware and equipment inadequacies and the continued

dependence on compensatory measures.

While no Conditions

Adverse to Quality were identified, the Audit concluded that

some of the equipment was obsolete and restricted the

effectiveness of the security program.

NRC has ascessed the

Safeguards Event Logs, pursuant to 10 CFR 73.71, and found that

nearly 93% of the logged security incidents are attributable tc

failed alarms, cameras, computers and coded-key card readers.

The same assessment noted a minor reduction in the number of

compensatory measures, due to the correct prioritization of work

requests and a relatively short turnaround time for repair of

security equipment.

It is noted that the licensee-identified

,

violations for officers being found inattentive to duty have a

'

direct relationship to the extensive use of compensatory

measures.

Much of the security equipment was poorly designed

and installed, and has over the years fallen into a state of

disrepair such that replacement parts are not always readily

available.

The NRC found several examples where vendor

furnished parts needed to be extensively altered before being

!

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41

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used in the current security system.

In the interim, the

licensee implemented appropriate compensatory measures.

At the Corporate level, the licensee continued to experience

attrition at its senior security management level. During this

' assessment period the ninth manager in the last 10 years re-

signed.

As a result of this continued turnover, numerous

-

assessments, evaluations and studies have been conducted with

correspondingly few corrective action programs reaching fruition.

After appointment of the most recent and current managers the

NRC can now begin to see significant progress made on several

old projects, some of which have been successfully completed.

In July 1988, the licensee finalized the reorganization of its

Corporate Nuclear Security Services Branch so that there now

exists a centralized (and accountable) management system.

Within this Branch there is a security compliance section, a

consolidated plant access and screening unit, a separate section

responsible for equipment upgrade and another section tasked

with plans and procedures.

A key element of the Branch is a

Safeguards Information Network which will computerize all site

and corporate data.

Another indication of improvement is the

upgrading of security training and increased tactical exercises,

Multiple Integrated Laser Engagement System (MILES) is available

to add to the realism of these drills.

The licensee's canine

corp is recogniz.ed by other federal and state agencies for its

expertise in detecting contraband.

At the site level, there exists a direct management matrix from

the Site Security Managcr to the Corporate Manager of Protective

Services within the Nuclear Power Group. The Site Director and

the Plant Manager have been instrumental in c'edicating site

support to reduce the number of security compensatory measures.

L

While technically there is a matrixed relationship between the

site and its security organization there is a very strong

matrixed interface.

Changu to Physical Security, Contingency, and Cuard Training

and Qualification Plans were generally well-prepared and

coordinated, with one exceptior..

The licensee withdrew one

revision to the Physical Security Plan when it was discovered to

contain a number of errors and omissions. The licensee has been

very responsive to questions and concerns raised on licensing

submittals.

The NRC has noticed an improvement in the quality of the

security staff while the size of the staff has been reduced.

This is evidenced in such key elements as training and

procedural knowledge.

There now appears to be a premeditated

implementation of the security program, as opposed to a reactive

security program.

l

___- ______-_____-__-_ - _ ~

.

.

'

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.

42

-

p

,

No violations were identified:

.

!

2.

Performance Rating:

l'

Category 2

3.

Recommendations:

The Board recommends that the licensee review it's security

upgrade priorities at all three facilities to ensure that the

Sequoyah security program continues to reduce its long term

reliance on compensatory measures in lieu of reliable security

equipment and systems.

F.

Engineering / Technical Support

1.

Analysis

NRC involvement in the engineering and technical support area

was more comprehensive than normally applied to licensee

activities.

This resulted from interactions between NRC OSP

and the licensee necessary to achieve acceptable engineering

resolutions as described previously in the summary section and

the technical complexity of many of the engineering issues.

The Engineering / Technical Support functional crea eccresses the

adequacy of the technical and engineering support for all plant

activities.

To determine the adequacy of the suppcrt previded,

specific attention was given to assurance of quality, includir.g

management involvement and control, the identification and

approach to resolution of technical issues, respersiveness to

NRC initiatives,

enforcement history,

opera tior,al

and

construction events, staffing, and effectiveness cf training,

and qualification.

This area includes all licensee activities

,

associated with design baseline evaluation irrplcr.:entation in

terms of Sequoyah plant modifications, engineering and

technical support provided for operations, maintenance,

surveillance,

training,

procurement,

and

configuration,

management.

This evaluation was based on Sequoyah site

inspections conducted by the NRC staff in the above areas and on

licensee technical submittals reviewed by the staff containir.g

engineering evaluations . supporting the Sequoyah Nuclear

Performance Plan (SNPP).

.

Inadequacies during the basis period were in the areas of design

analysis, modification control, engineering docume nta tion ,

design basis utilization, and design verification.

In order to

correct these weaknesses, TVA senior management increased their

involvement and control during this assessment period to improve

the quality of engineering support.

TVA nanagement involvement

was demonstrated through issues including; the Replacement Items

Prngram, in which TVA Corporate and Sequoyah management were

greatly involved in the program to ensure immediate and effective

corrective action; the issuance and use of procedures in the

civil / structural area, including pipe supports and restraints;

___ _ _ __ - _ - _ _ - _ - _ - _ _ _ _ _ _ - _ _ _ _ _ _ _ _ _ _ - _ .

- _

-

_

_

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_

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.43

'

.

'the drawing: control' process,.which is considered .now to be .of

~

Io

' high quality and. accuracy; and the procedures .for control: of

I

thermal expansion tests.

The procedures used for the thermal

expansion tests were well defined and explicit, demonstrating

evidence of prior planning with a proper assignment of

priorities.

,

In . response to ' concerns expressed by the NRC, TVA revised

Sequoyah's snubber surveillance program procedures, resulting in

a- more conservative selection.of the number of snubbers to be

tested upon occurrence of test failures.

-TVA DNE continued the control of the EQ activities as had been

established in 1986 and 1987.

During thisLassessment period,

Sequoyah'transitioned from a separate dedicated EQ' organization

to a matrix organization within the site DNE organization. This

transition appeared to occur without interruption or degradation

of the quality of DriE support to the plant.

Engineering

decisions were made at appropriate levels.

This is'a clear

example' of TVA . DNE management involvement and control in

assuring quality.

Other issues in which DNE management oversight and involvement

was 'strongly prevalent included DNE representation during the

morning and outage planning meetings, the initiation cf a duty

DNE manager for weekend and back shift engineering support for

.

Op.erations, and the direct management involvement in the

'

organization.and allocation of resources for the P,estart Test

Program.

-

TVA DNE management, hoviever, has not been adequately involved to

provided in Generic Letter (GL) specifically, the staff guidance

ensure quality in all cases.

S

1

86-10, for spurious actuations

from high-impedance faults had not been followed by TVA.

Similar problems with 'the implementation and ' applicability of

other portions of GL 86-10 had been previously discussed with

the licensee early in the assessment period.

This instance

indicated a reliance of the licensee on the NRC to establish an

adequate scope and content for this generic letter with respect

j

to the extent of applicability and indicated a lack of

,

!

responsiveness to this NRC initiative.

'

TVA did not follow their design commitments made to the NRC

involving criteria for pipe supports and piping analyses. These

i

cases indicated a lack of management involvement in the

activities they supervise and a lack of quality verification for

I

commitments made to the NRC.

,

TVA experienced problems in engineering documentation adequacy

)

and in the backlog of open plant change packages.

For example,

TVA did not properly document changes to the Emergency Diesel

i

__- ___ _ _ - _

.

,

_

_

_

__ _ _ - _ _ - _ - _ - -

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44

.

Generator (EDG) 2B-B load analysis (SQN-E3-002) from Rev'ision 7,

which was used as the' basis for Unit 2 restart, to Revision 10,

in which all EDGs were analyzed. for Unit 1~ restart.

Revision

10 which documented that EDG 28-B had reduced diesel generator

loading,~ 1acked complete information and required additional

supporting data to explain the leading changes.

'Furthermore,

the summary letter of EDG load analysis dated August 11, 1988.

contained three incorrect-numbers, only'_one of which was later

identified by TVA.

NRC staff discussions with modification

- personnel revealed there were approximately 1300 engineering

design change workplans: remaining open, some dating back to

1980.

All required physical work was completed on these work-

plans prior to plant startup, however, the workplans were

'left open!for various reasor.s. These problems indicate lack of

quality, verification for submittals made to the NRC and a lack-of

management'_invoiva ent.

The approaches taken by the site end corporate engineering-

staffs to resolve technical issues from a safety standpoint were

adequate with improvement shcwn during the assessment period.

For example, in the civil / structural area, the staff reviewed

- TVA's submittals for justifying the adequacy _of Interim (or.-

Restart) Criteria and design calculations for a. field erected

~

tank, cable tray supports, pipe supports, conduit and supports,

ERCU pipe access cells, the ERCW pump station, masonry walls,

.the steel . containment vessel, equipment supports and miscel-

.

laneous civil / structural issues, and found that the engineering

records and design calculations were generally complete end

documented.

However, as a result of NRC reviews, some of the

design calculations were regenerated two cr three times by TVA

before lVA was able to r'eet and implement restart requirement

design criteria which was acceptable to the NRC. The evaluation

results for' the issues' iden:1fied were' reascnable, logical and

-

net the Sequoyah restart requirements.

In the area of pipe

supports, cable tray supports, pipe restraints and equipment

supports, staff review ano evaluation found that there was a

defined set of procedures for the control of engineering

activities.

It was concluded that engineering records were

available, relatively easy to access and were clear.

Minor

errors were found in some of the specific calculation packages

reviewed, however, the general assessment was that TVA had

improved the quality of the results of the engineering and

technical support groups.

TVA engineering personnel were found to have an understanding of

!

the issues involved when evaluating changes to the facility.

The staff audited the licensee's report required under 10 CFR 50.59 supporting the seismic qualification of the interim and

'

final designs associated with the component cooling water (CCW)

heat exchanger replacement and associated piping modifications.

- _-__

_

__ _ -

_ _ _ - _ - _ _ _

- _ -

_ - _ _

- _ _ .

- - _

._ _ _ _

,

. - -

_ _ _

_ - _ - - - - - _ _

d

.

45

-

The detailed analyses provided to the staff exhibited a

comprehensive evaluation of the CCW system to justify continued

operation of Unit I while the piping modifications were being

implemented.

The engineering records were extensively

documented and readily available for staff audit. The licensee

exhibited a thorough understanding of the technical analyses and

clearly explained the rationale for allowing continued operation

of Unit 1 during the CCW heat exchanger changeout.

Further examples of adequate TVA engineering reviews included

the piping thermal expansion test program which demonstrated a

sound and thorough approach to identifying potential inter-

ference to piping thermal growth as a result of implementation

of plant modifications.

Also, TVA's response to the staff's

concerns regarding potential damage to the containment during

the Sequoyah extended shutdown period demonstrated a sound

approach to resolving the staff's concerns.

However, in several instances during the assessment period, TVA

actions indicated an inconsistency in the thoroughness of

technical resolutions and a lack of attention to detail.

Examples of weak technical resolutions and lack of thoroughness

included TVA's initial cable testing program, EDG voltage

analysis (SQN-E3-011, Revision 2,) and a proposed TS change

which applied to the Turbine Driven Auxiliary Feedwater Pump.

(TDAFWP).

TVA demonstrated a general understanding of the

safety issues' involved, however, the engineering analysis

accompanying these issues did not reflect an indepth review of

all applicable safety aspects.

The DNE effort supporting the

Sequoyah Unit 2 pressurizer safety valve steam trim / leakage

resolution was another exmple of a lack of effective DNE action

to resolve plant problems.

The staff audited the licensee's modification to correct a

deficiency in the teismic qualification of Bailey Meter elec-

trical_ instrumentation cabinets involving the use of aircraft

cable.

The staff found the licensee's modification to be

unacceptable.

The licensee did not demonstrate an under-

i

standing of the seismic qualification requirements for the

Bailey Meter cabinets and thus its fix, using aircraft cable,

j

was not sound.

In addition, only after the modification using

i

the aircraft cable was found to be unacceptable, did the

f

licensee establish that the electrical instrumentation was not

required for safe shutdown.

'

While the level of cooperation between DNE and plant personnel

has substantially improved, the technical adequacy of the

engineering support has not been of a consistently high level.

While progress over the assessment period was evident, errors

and incomplete evaluations have continued.

-

_ _ _ _

_ _ _ - _

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.;

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46

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g

' During the assessment period, tha licensee generally responded

well to NRC initiatives.

While NRC'had to. insist on cable type

'

-

testing, TVA has since been responsive in all remaining areas of

H

'

the cable testing program. . Other examples of TVA's responsive-

ness .were demonstrated in the ' area of procurement.

In.a few -

Leases (e.g. molded case circuit. breakers) Sequoyah engineering-

l

l

staff exceeded reporting requirements to the NRC with respect to

reporting the s_ cope of problems. ThisJ assisted the NHC in

!

providing up-to-date. guidance to other licensees..'In the area

!

'of fire protection,- responses to NRC requests have generally -

>

been timely as well;as thorough except for certain provisions of

GL 86-10.

An exception was_in the area'of~ establishing welding

>

inspector certification where records were not complete nor well

maintained and corrective action was not timely.

Other respon-

i

'

sive efforts worth noting include the timely corrective action

taken for problems identified during the pre-operational thermal

j

expansion- test program.

These efforts represented timely

corrective action implementation for an NRC initiative which

i

went beyond minimum NRC requirements and, with TVA's proper

completion - of = the test program, significantly enhanced the

reliability of the Sequoyah piping systems.

During the assessment period two violations were issued in the

!

'

Engineering / Technical Support area.

The first violation was for

failure to take adequate corrective action and follow procedures

relative to dedication of commercial grade items for use in

safety-related applications.

While NRC had observed improve-

l

i

ments in TVA's procurement of purchased parts due to previous

corrective actions, the inspection determined that Sequoyah was

still procuring commercial grade parts without adequate

H

dedication of the parts for use in safety-related applications.

j

The second violation documented that TVA did not have hydraulic

-j

. and thermal design calculations for the containment spray

l

+

system, which estcalished the design basis for the pressure ard

temperature bourcaries.

Corrective actions for both of the

above violations have been implemented and were determined

edequate.

Operational and construction events which involved TVA

)

engineering have been properly reported to the staff via the

Licensee Event Reporting system.

Engineering support for these

,

occasions was adequate to support both proposed and implemented

j

corrective actions.

!

l

'

TVA staffing levels in the engineering / technical support area,

including management, were adequate.

Position identifications

I

and definitions of authority and responsibility were well

established and managed during the assessment period.

In the

civil / structural engineering area, the items that required

resolution by TVA engineering from the NRC's Safety System

l

_ _ _ _ - - _ _ _ __

_

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47

.

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Quality Evaluation, were in some instances delayed because of

'

lack of available staff.

However, this was noted as an

exception rather than the norm.'

9

The effectiveness of TVA's training and qualification programs

in engineering and technical support has generally been adequate

with a few exceptions.

Lack of adequate training was a major

cause of a violation in the procurement area.

A lack of

adequate training in administrative procedures was found to

j

be a major contributing factor in ISI training and documentation

j

problems and in the reluctance by the ISI group members who

performed radiography on welds to follow administrative

requirements for procedure changes.

These events were

inconsistent with the observed results of training for other TVA

organizations (e.g. plant modification training, maintenance

craft training, and Shif t Technical Advisor and Operator

training).

The pre-operational thermal expansion test program

engineers were noted as being well trained ano qualified for the

i

performance of their required duties.

In general, the training

and qualification programs contributed to an adequate under-

standing of work and general adherence to procedures. The number

of exceptions were acceptable.

Management of the training and

qualification program within the ISI area was inadequate in that

adherence to administrative procedures was not enforced.

Two violations were identified:

a.

Severity Lesel IV violation for failure to take adequate

corrective acticn and follow procedures relative to

dedication of commercial grade items for use in safety-

related applications. (88-07-01)

b.

Severity Level IV violation for failure to hase hydraulic

and thermal design calculations for the cont 6inment spray

system. (88-29-01)

2.

Performance Rating:

Category: 3 Improving

3.

Recommendations:

The Board is encouraged by the initiative and efforts expendeo

by TVA to improve the quality and effectiveness of its

engineering suppcrt for the Sequoyah Nuclear Plant.

The Board

,

recognizes that a significant amount of complex engineering work

was completed.

Since considerable NRC effort and input was

'

needed to obtain acceptable engineering resolutions, the 00ard

concluded that TVA has not yet demonstrated independent

performance at a level greater than that necessary to meet

minimum regulatory requirements.

The Ecard recoiserds that

!

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48

)

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i

management attention to this area continue, that those long term

j

commitments made ' to assure continued improvement after the

'

initial restart of both units be completed as scheduled, and

that adequate long term staffing and funding be maintained to

i,

'

support completion of the long term commitments.

G.

S_afety Assessment / Quality Verification

1.

Analysis

The area of Safety Assessment / Quality Verification included

quality assurance and the corrective action process, safety

committees, the 10 CFR 50.59 safety evaluation program, event

reporting and root cause assessment, the employee concerns

program, licensing activities, and corporate support for quality

verification.

The most significant improvement *las i~n the

corrective action program which is now functioning adequately.

Improvements were ncted in safety committee performance and root

cause assessment.

Weaknesses were noted in the 10 CFR 50.59

safety evaluation program.

While both site and corporate management were involved in the CA

area and the policies were adequately stated, NRC inspections

and other NRC staff reviews and evaluations indicated that all

new policies were not fully understood by Seoucyah personnel.

Problems continued to exist during the early part of the rating

period in the corrective action process and cdequate corrective

action was occasionally not effective resulting in repetitive

CAQRs.

In addition, CAQR resolutions were sometimes delayed.

Changes to the QA topical report are requirea to be submitted to

the NRC at least yearly.

TVA made several extension requests

for submittal of changes indicating a slow approval process end

a reliance on the NRC to establish an adequate time frame for

submittal. * While the violations that occurred during the

assessment period have not been directly related to the QA

program, they have involved failure to follow procedures or

failure to take adequate corrective action.

Key positions in the QA department were identified and

authorities and responsibilities were well defined.

The staff

expertise level was considered excellent.

Trcining contributed

to an adequate understanding of the QA prcgram.

The licensee continued the implementation of the CAQR program

which was established during the basis pericd.

Early in the

'

assessment period CAQR reviews indicated weaknesses in opera-

bility and significance determinations, reviewer and management

training, timeliness, documentation, and auditability of re-

cores. The Sequoyah Site Deputy Director personally took charge

of the implementation of the Sequoyah CAQR program to ensure

that implementation problems would be resolved.

The CAOR

. _ _

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1

process required an encrmous amount of dedicated upper nanage-

ment effort to ensure that it contir:ued to function adequately.

.One

major reason that the dedicated management attention was

i

necessary was that a large number of issues were identified at

,

!

Sequoyah, and at other TVA plants which had implications on

Sequoyah, that required resolution through the corrective action

program, resulting in a significant CAQR backlog.

A second

reason was that time-sensitive equipment operabilty determina-

tions en engineering issues required determinations prior to the

completion of the CAQR technical evaluations resulting in the

required use of large amounts of predecisional information. The

i

corrective action process was determined to be adequate to allow

the restart of both units.

To this end an order, which dealt

with a management breakdown in controls fcr safety concerns

having generic implications to other TVA sites, was considered

adequately resolved for Sequoyah.

In order to reduce the amount of dedicated upper nanagement

effort necessary to make the CAQR system work, the licensee

developed a change to the CAQR process and implemented it in

September 1988, immediately prior to the restart of Unit 1.

The

change provided several administrative control programs to act

ds Corrective action screening processes. Those issues that did

not meet the acceptance criteria for being a CAQR stayed in the

administrative control programs for resolution.

A Quality

Verification Inspection (QVI) conducted near the end o' the

-

assessment period fcund that the changes were adequately

implemented and strongly supported by ser.ior line n;anagement.

The char.ges appeared to have the desired effcct of forcing

insignificant and less significant issues down to the proper

level for resolution, while keeping safety significant items at

the senior management level.

The QVI reviewed for quality and quality verification in the

areas of plant operations, surveillance, maintenance, corrective

actions,* modifications, and implementation of commitments made

to the NRC.

The QVI concluded that site line management was

strongly dedicated to quality and was convincing workers that

quality work was what was expected.

One exception to this

attitude was in the radwaste processing area as revealed by a

resin transfer event that occurred at the end of the assessment

period. This event indicated that management attention had been

lacking in the radwaste processing area and that overall site

procedure upgrades had not had an effect on upgrading quality in

this area.

The function c' the quality monitoring organization was to

assist site management in meeting quality objectives by

identifying ccr.ditions adverse to quality on a real-time basis

before they impacted on nuclear safety, reliability, or

_ _ _ . _ _ _ _ _

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7

50

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component' operability.

The quality monitoring organization was

observed to be a well qualified and adequately staffed

organization which was adequately performing its function.

The use of interfaces between groups, by the organization as a

whole, to verify and accept quality when deliverables were

trar,sferred was not emphasized as a quality verification tool.

For example, the maintenance department was using an interface

organization between the shops and QA to ensure that completed

surveillance tests represented quality work prior to their

transfer to QA for review, however some of the problems that

were being identified for correction had resulted because

procedure changes had not been adequately communicated to the

shop organization responsible for perfchaine them. An interface

problem was also identified between engineering and the plant in

relation to vendor manuals having conflicting data and resulted

from a lack of communication between the two organizations.

Although interface problems between engineering and the plant

were identified by the NRC staff during the basis period, inter-

faces were-not actively used by site or corporate mar,agement for

the purpose of quality verification.

The licensee identified that the percentage of Boron-10 isotope

in the boron being added to the reactor coolant was outside of

the established procurer:ent and design specifications.

Although

this and related nonconforming ccnditions were identified by

licensee personnel on at least three distinct occasiens, the

established corrective action process ecs not implemented in a

timely manner and was only initiated after the issue was raised

by the NRC. Once identified by the licensee, corrective actient

were adequate.

The licensee's 10 CFR 50.59 program was reviewed and in most

cases found to comply with minimum regulatory requirements,

however weaknesses were identified.

The first weakness was

identified as a violation and related to non-conservative

translation of regulatory requirements into procedures; the

second weakness was related to the lack of qualification

requirements for the performance of screening reviews; the third

weakness was related to a lack of definition for when

interdisciplinary reviews were required, and the fourth weakness

was related to coordination of the reviews between groups.

These weaknesses indicated minimal management involvement in

assuring the quality of this function.

In addition, a failure

of the 10 CFR 50.59 process was identified in relation to the

excessive post trip cooldown effect on shutdown margin which was

,

identified early in the assessment period and issued after the

end of the assessment period as a Severity 1.evel III violation.

1

A reorganization of the Plant Operations Review Staff (PORS),

'

i

which is responsible for reporting and investigating plant

'

events, occurred at the beginning of the assessment period.

NRC

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51

..

concerns about inadeouate root cause analysis for- plant events

were addressed by prcviding training for the PCRS staff.

Root

cause determinations and licensee corrective actions improved

throughout the SALP period and have becore more reliable and

technically correct near the end of the period. One failure of

the root cause reviews was in the area of excessive post trip

'

cooldowns and the resulting effect on end-of-life shutdown

margin which was issued after the end of the assessment period

as a Severity Level 111 violation.

The objective for ISEG and the other safety review committees to

identify underlyinc problems before they become issues was

recognized by TVA management.

The safety comnrittee reorganiza-

tions which occurred near the end of the basis perioc began to

have an effect in accomplishing that objective during the

assessment period.

PORC was more aggressive and technically

involved in the resolution of issues affecting the safe

operation of the units.

PORC improvements were due to

consistency in perscnnel staffing, strong leadership from the

new plant manager, and use of the Plant Operations Review Staff

(PORS) as a part-time support group for PORC.

FORS employed

specialized training end skills to perform root cause

evaluations and determine corrective action plans associated

with plant events, which were then submitted a:. completed

projects te PORC.

The use of the P0RS to perform investigative

data gathering and initial evaluat. ions has allowed PORC to be

more deeply involved in day-to-day plant eversight.

The NSRB

'

has continued to chcw a low profile with respect to crisite

ectivities functioning principally in the areas of LER

evaluation, TS change approval and cther area:: that allow fcr

offsite review.

The ISEG was reorganized as a result of a

TS change and became more aware of industry issues, showed a

greater presence in the plant, and by the end of the assessment

period, was becoming an effective auditor of piant activities.

Near the end of the period, ISEG and the other safety committees

were working together better in understanding what each of their

roles should be in accomplishing the overall objective.

j

l

A broad spectrum of safety issues was identified by TVA

employees in the ECTG program which reflected a previous lack of

management involvement with quality.

The NRC staff review of

the Sequoyah ECTG investigations, corrective actions, and

planned programmatic improvements concluded that the evaluations

were generally adequate and well documented.

I

i

I

The Employee Concerns Program (ECP) continued to be implemented

in an impressive and professional rcnner.

Several audits cf ECP

open files ar.c' concerns were completed with no significant

1

l

findings or wealnesses.

Restart determinations performed on

open files and concerns were accurate and conservative.

Followup on issues which were both NRC issues and ECP issues

]

_ _ _ _ _ . _

_ _ _ _ _ _ _

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52

.

,

resulted in parallel, conservative conclusions.

The ECP

encouraged the return of issues to line managenent for

resolution ar.d in dolng so, has strengthened line inanagement

responsiveness to issues identified by non-canagement employees.

There was a tremendous amount of activity in the licensing area.

Supplemental information regarding licensing ectivity is

provided in Section F, under Supporting Data and Summmaries.

Generally, the large majority of the work done by TVA on

licensing issues was good and showed evidence cf prior plenning

by management.

Hcwever, TVA had a tendency to be optimistic in

'

establishing submittal dates which has resulted in frequent

i

requests for extensions.

Ir. addition, two examples, TSCR 87-47,

Control Poom Emerger.cy Ventilation System, and ISCR CC-21, River

Water Level and Temperature, were noted where TVA knew that a TS

l

change would be needed and the submittals were not made on a

timely basis,

Submittals by TVA generally shcwed an understanding of the

i

'

technical issues beinD discussed.

The approach to the technical

l

issues exhibited conservatism and were viable, thorough, and

j

generally sound as demonstrated in their quick response to a

l

primary to secondary leak that developed in a Unit 2 steam

generator during start-up, in their response to hCC Eulletin

88-02, " Rapidly Propagating Tatigue Cracks in Steam Gercrator

Tubes", and in their sube ttals requesting relie' from ASNE code

d

Section XI, inservice Inspection and Operating Plant Cece.

In

additicn, TWs proposal tc revise ira;trument accuracy

calculations for the PCP undervoitage reactor protection channel

in TSCR 87-18, RCP uncervoltege reactcr trip, could Le censidertd

illustrative of a rigorous evaluation cf technical problems and

a timely update consistent with ir.dustry practice.

This,

however, was t.ot true for TSCR 88-T0, Upper lieed Injectinn

Accumulator Level Switch Setpoint which was submitted without

TVA understanding thet its application dia net meet 10 Cfh

50.46(a)(1) and therefore required an exarption.

Conservatism in the licensee's alternate approach tc problems

was generally exhibited and decisicn making was usually at a

level that ensured adequete managerent review.

The technical

reviews occasicnbily were lecting in detail and/cr technical

basis.

Licensee statements at meetings were not always well

thought cut prior to presentation to the NRC indicating that

communication between licensee organizations was not always

clear.

TVA was generally responsive to NRC initiatives.

NRC

expectations regarding the issue of Ste6m Binding of Acxiliary

Feedwater (AFW) pumps were met in the area of technical accuracy

and were exceeded in the area of scheduling.

The overall

_

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staffing to support operating activities was adequate with the

>y.

licensing engineer-being well qualified and adequately trained.

- The site licensing organization has been successful in improving-

1

h

. the timeliness and quality of responses to NRC violations.

TVA Nuclear Power cor) orate management was usually involved in

'

Sequoyah site activit'es in an effective manner.

The corporate

level was reorganized on-~ July 1,1988, as part of a general

reorganization of TVA itself, and resulted in a reduction in the

number of levels of management between the Senior Vice President-

Nuclear Power, who is manager of the TVA nuclear power program,

and the site.

Also, the manager of the TVA nuclear power

program, who was a contract employee, was replaced by a perma-

nent TVA employee.

The emphasis of TVA's nuclear power program

has switched.to operating the Sequoyah units within constrained

TVA budgets, compared to past budgets, and reduction-in-force

within TVA's nuclear power program including the site.

The

effects of the new emphasis is ur.certain, however, the NRC has

noted that TVA was reassessing the' dates and scope for commit-

ments.

Corporate support for site activities was observed in the areas

of Operations, Quality Assurance, and outage inanagement.

The

support in these areas was limited to activities and managers

necessary . to support the restart of Units 1 and 2 and the

refueling of Unit 2.

The support was not global in nature and

consisted mainly of loaned corporate managers and specialists

.

that met specified needs.

Activities appeared to be well

supported by corpor~ ate management and the mai. agers supplied by

corporate management were professional and well suited to the

assigned tasks.

A site Radiological Assessor position has been

established.

The position

reports

to the Manager of

Radiological Control, a corporate position rather than to the

Site Director. The position provides a programmatic cverview of

the- Sequoyah radiological control program and an independent

reporting path offsite.

The Site / Corporate interface was

adequate and programmatic overview of the site was occurring.

For the assessment period, ccrporate mt.negement continued to be

generally responsive to NRC initiatives.

The responses to NRC

were generally timely, sound and thorough. /ilthough Unit I was

restarted in November 1988, the restart date was only three

months later than originally scheduled by TVA, as compared to

(.

two years later for Unit 2, which showed evidence of improved

L

planning and assignment of priorities.

.The significant exceptions to TVA's general responsiveness to

NRC initiatives and timely submittals in the rating period were

the resolution of the silicone rubber insulated cable testing

issue and the tardiness of TVA in submitting Revision E of the

Corporate Nuclear Performance Plan to reflect the July 1,1988

reorganization.

.

I

_ _ _ _ _ _ _ _ _ . _ _ _ . _ _ _ . . . . , _ . . _,

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54

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Seven violations were identified:

a.

Severity Level IV violation for failure to follow

procedures for authorization to exceed plant overtime

limits.(327,328/87-70-01)

b.

Severity Level IV violation for failure to follow

procedures for installation and inspection of seal table

bolts. (327, 328/88-09-01)

c.

Severity Level IV violation for failure to take prompt

corrective action for deficiencies in QA record storage.

(327,328/88-09-02)

l

d.

Severity Leve'l IV violation for failure to properly

translate 10 CFR 50.59 requirements into instructions or

procedures.

(327,328/88-43-01)

e..

Severity Level IV violation for failure to take adequate

corrective action for prevention of reactivity changes

while both trains of control room ventilation are

inoperable. (88-27-01)

!

f.

Severity Level IV violation for failure to. take adequate

'

corrective action to preclude repetition of violation

87-S0-01 involving lack of control over plant evolutions,

,

and system and equipment status in the radioactive weste

-

area.

(88-50-01)

g.

Severity Level IV violation for three examples of failure

to promptly identify and initiate adequate corrective

action for Boron-10 procurement problems.

(88-60-01)

l

2.

Performance Rating

' Category: 2

3.

Recommendations

None

j

V.

SUPPORTING DATA AND SUMMARIES

l

A.

Investigation Review

The NRC's Office of Investigations closed fourteen cases which dealt

with TVA during the assessrrent period.

None of these involved

enforcement action pertaining to Sequcyah.

l

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B..

Escalated Enforcement Action

1.

Civil Penalties

4

Severity Level III violation issued on July 3,1988, concerning

failure to ccmply with TS when both centrifugal charging pumps

were inoperable and failure to report this condition pursuant to

10 CFR 50.72. ($50,000 CP)

,.

2.

Discretionary Enforcement for Shutdown Plants

Failure to meet the 10 CFP 50.59 requirements for a 1984

auxiliary feedwater pump modification.

No Notice of Violation

or Civil Penalty was issued as discussed in a letter dated

May 9, 1988.

C.

Licensee Conferences Held During Appraisal Period

During the appraisal period, meetings were held with the licensee to

discuss various issues, as follows:

1. Management Meetings

Date

Purpose

February 11, 1988

Meeting to discuss load sequencing of

plant diesel generators.

March 09, 1988

Meeting to discuss technical issues related

to 10 CFR 50 Appendix R.

April 14, 1988

Meeting to discuss differences between

Sequoyah, Units 1 and 2 in the Sequoyah

Nuclear Performance Plcn.

April 29, 1988

Meeting to discuss (1) the Unit 2 steam

generator tube leakage and (2) loop seals

.

'

for the pressurizer safety valves.

June 13, 1988

l'eeting to discuss the restart of Unit 2 in

light of the five scrams from power in

May 1988.

June 22, 1988

Meeting to discuss the TVA commitments for

Unit ?.

July 21, 1988

Meeting to discuss Phase II of the Design

Baseline and Verification Program fcr

Sequoyah.

September 8, 1988

Meeting to discuss changes to the TVA

Conditions Adverse to Quality Program at

-

Sequoyah.

_ _

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56

September 13, 1988 Meeting to discuss TVA's preparation for

Unit I restart and the post-trip cooldown

shutdown margin issue.

September 15, 1988 Meeting on TVA's Microbiological 1y

Induced Corrosion Program at Sequoyah.

October 24, 1988

Meeting on the status of TVA's commitments

to NRC on Sequoyah.

November 28, 1988

Meeting on the Essential Raw Cooling Water

pumphouse formulation and roadway access

'.

cells.

2.

Enforcement Conferences

March 17, 1988

Enforcement

Conference

at

Sequoyah

concerning

centrifugal

charging

pump

operability which resulted in EA 88-86.

(IR 88-20)

July 28, 1988

Enforcement Conference at Sequoyah

concerning upper head injection system

operability. Issued as Severity Level IV.

(IR88-34)

December 19, 1988

Enforcement Conference at NRC Headquarters

concerning the affect of excessive cooldewns

following reactor trips on end-of-life

shutdown margin which resulted in EA 88-307.

(IR 88-35 & 88-55)

D.

Confirmation of Action Letters

1.

April 26, 1988

Reinstatement of Hold Points for

Unit 2 Restart from Steam Generator

Outage

2.

June 16, 1988

Confirmation of Release from Unit 2

Hold Points

3.

November 7, 1988

Reinstatement of Unit 1 Mode 2 Hold

Point

a

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57

E.

Review of Licensee Event Reports

During the assessment period, there were a total of 78 LERs analyzed

for Units 1 & 2.

The distribution of these reports by causes, as

determined by the hRC staff was as follows:

LER CAUSES

UNIT 1

UNIT 2

Component failure

................. 2

6

Design ............................ 2

1

Construction / Installation /.......... 1

3

Fabrication

Inadequate Procedure...............

11

3

Test Calibration....................

7

3

0ther...............................

7

3

Personnel

- operati ng acti vity. . . . . . . . . . . . . . . . 5

6

- maintenance activity..............

2

4

- test / calibration..................

2

6

-

other.............................

3

1

Total

42

36

F.

Licensing Activities

The assessment of licensing activities was based, in part, upon

licensing actions successfully completed duri,ng this period.

These

include the following:

-

1.

Discretionary Enforcement /ilaiver of Compliance

January 30, 1989

Emergency Diesel Generator Surveillance

Testing

2.

Reliefs Granted

February 8,1988

American Society of flechanical

Engineers (ASME) Code Case N-411

May 11, 1988

ASME Code Section XI Relief for the

Microbiologically Induced Corrosion

(MIC) Program

August 18, 1988

Hydrogen Analyzer Sampling Valves,

ASf1E Code.Section XI Relief

September 15, 1988

ERCW Valves on CSS Heat Exchangers,

ASME Code Section XI Relief

September 15, 1988

Generic Relief on Use of Ultrasonic

Monitoring of Pump Flow

November 4, 1988

Temporary Deviation from Appendix R to

to 10 CFR 50, Section III.G.

.

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_ _ _ - _ _ _ _

.

-___--_ -_ - __ -

_

c.-

,

-.

58

-

3.

Exemptions

July 14,_1988

Schedular Exemption to Appendix J,

Type B and C Testing

September 22, 1988

Exemption to Appendix J. Type C

-Testing for C/RHR Spray System Check

Valves

October 26, 1988

Temporary Exemption to Appendix K ECCS

Calculations to May 31, 1989

January 26, 1989

Exemption to 10 CFR 50.46(a)(1),

Approved ECCS Analysis for Operating-

Cycle 4

4.

Orders

March 31, 1988

Modification of Order 85-49 stating

that Sequoyah had satisfied the

requirements of the Order.

5.

Emergency or Exioent Technical Specification (TS) Amendments,

June 30, 1988

Exigent TS /cendment on Ct rporate -

-

Reorganization

January 3'0, 1989

Emergency TS Amendment on Diesel

Generator Surveillance Testing

6.

Malti-Plant Actions (MPA) Resolved

Date

MPA Description

fiarch:21, 1988

F-05, Procedures Generation Package

May 5, 1988

A-21, Pressurized Thermal Shock

May 18, 1988

B-60, Environmental Qualification

for Unit 2

July 20, 1988

B-98,Bulletin 85-01, Steam Binding of

AFW Pumps

September 9, 1988

B-101, Boric Acid Corrosion of Carbon

Steel RCS Components

November 28, 1988

B-81, GL 83-28, Items 4.2.1/4.2.2

February 3, 1989

B-60, Environmental Qualification for

Unit 1

_

.

' -

_ _ _ _ _ . _ _ _ _ _ _ _ _ _ _ _ . _ _ _ _

. _ _ _ _ _ _ - . ._ ______

'

..

,

l

59

7.

Significant Plant-Specific Issues Resolved

Date

Description

February 23, 1988

Sequoyah Pipe Support Criteria

February 23, 1988

Unit 2 Extended Heatup Prior to Restart

March 11, 1988

Unit 2 Restart Employee Concern Element

Reports

March 14, 1988

Revised Sequoyah IST Program

March 21, 1988

Hydrogen Analyzer Operability

May 18, 1988

NUREG-1232, Volume 2, Review of

Sequoyah Nuclear Performance Plan for

Unit 2 Restart

May 25, 1988

Silicone Rubber Insulated Cable Inside

Containment

June 23, 1988

Bulletin 86-02, Static-0-Ring Switches

Jul.y 6, 1988

GL 87-06, Periodic Verification of PIV

Leak Tight Integrity

August 3, 1988

10 CFR 2.206 Petition on Emergercy

Diesel Generators

September 22, 1988

JC0 for Operation with C/RHR Spray

System Check Valves without

_

Appendix J, Type C Testing

November 4, 1988

Unit 1 Restart and Both Units

Non-Restart Employee Concern Element

Reports

December 5, 1988

GL 87-12, Loss of RHR with RCS

Partially Filled

February 3,1989

NUREG-1232, Volume 2, Supplement i

Review of Sequovah Nuclear

Performance P'

for Unit 1 Restart

.

.

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8

-

- - -

_

.

.

63

i

,

G.

Enforcement Activity

,

l

All violations for the appraisal period were cited against Unit 1

and Unit 2.

NO. OF DEVIATIONS & VIOLATIONS IN SEVERITY LEVEL

FUNCTIONAL

AREA

DEV

V

IV

III

II

I

PLANT OPERATIONS

1

4

1

RADIOLOGICAL CONTROLS

2

MAINTENANCE /

1

16

SURYLILLANCE

EMERGENCY PREPAREDNESS

1

2

SECURITY

ENGINEERING / TECHNICAL

2

SUPPORT

SAFETY ASSESSMENT /

7

QUALITY VERIFICATION

TOTAL

1

2

33

1

H.

Reactor Trips

A total of seven automatic reactor trips occurred during the

assessment pericd, five above 15% power and two below 15% power.

No

manual trips were initiated and no trips occurred with the unit

~

subcritical.

In general, these reactor trips occurred during power

esca11ation activities ano were followed by extended periods cf

continued operation.

The trips are described in more detail below:

May 19,1988 - Unit 2 tripped from 73% pcwer due to a steam / feed

flow mismatch coincident with low steam generator level. This

situation occurred due to maintenance being performed concur-

rently on two p'ieces of equipment which together could cause a

reactor trip (one channel of steam generator level indication to

replace an unqualified splice and the #3 heater drain tank level

controller which resulted in plant oscillations).

May 23,1988 - Unit 2 tripped from 70% power due to low flow on

RCS Loop #4.

This situation occurred due to a personnel error

while performing a surveillance on the Icop #4 flow transmit-

ters.

June 6,1988 - Unit 2 tripped from 98% power on steam / feed flow

mismatch coincident with low level in li4 steam generator. The

trip occurred while performing a surveillcrce on the feedwater

regulating valves and resulted because a diode was missing in

the block circuit.

_

_ _ _ _ _ _ _ _ _ _ _ _ -

-

'

<

,

e

64

June 8, 1988 - Unit 2 tripped from 12% power on low-low level in

  1. 2 steam generator due to an operator error when placing the

feed pump controller in the automatic position resulting in

steam generator level oscillations.

June 9, 1988 - Unit 2 tripped from 20% power on low-low level in

  1. 2 steam generator due to feedwater heater isolations which

caused feed flow and steam generator level transients.

November 18,1988 - Unit 1 tripped from 72% power due to an

electrical ground in the main generator which tripped the main

turbine.

December 26,1988 - Unit 1 tripped from 75 power on low-low

level in #4 steam generator.

The trip was caused by a series of

events that started with a manual trip of the main turbine due

to generator seal rubbing.

After the turbine trip, steam

generator level was controlled using manual feedwater control

which resulted in a feedwater isolation from high-high level in

  1. 2 steam generator followed by the reactor trip on low-low level

in #4 steam generator.

I.

Effluent Release Summary

1985

19.86

1987

Gases

(Curies)

(Curies)

(Curies)

Fission and Activation

Gases

4.57 E+03

1.21 E-00

0.0

Halogens and

Particulate

6.63 E-03

1.56 E-03

5.04 E-04

Liquids

Fission and Activation

Products

2.08 E 00

1.65 E-01

4.66 E-01

Tritium

6.33 E+02

1.72 E+02

1.19 E+02

J.

Acronyms

As-Low-As-Reasonably-Achievable

ALARA

-

American Society of Mechanical Engineers

ASME

-

American National Standard Institute

ANSI

-

American Nuclear Insurer

ANI

-

AVO

-

Assistant Unit Operator

All Volatile Treatment

AVT

-

Condition Adverse to Quality

CAQR

-

, Component Cooling Water

CCW

-

.

, _ _ . _ . _ _ _ _ _

,

_

_

_

_

.

.

-..

.

.

!p .

c

65-

'

Contract [ngineeringGroup.

CEG

-

Nuclear Performance Plan

'

' NPP.-

-

Design Easeline Verification Program

'DBVP

-

Division of Nuclear Engineering

DNE.

-

Escalated Enforcement Action

EA

-

ECCS

~

Emergency Core Cooling-System

-

' Employee Concerns Program

ECP

-

Employee-Concerns Task Group

.ECTG

-

Emergency Diesel Generator

EDG

-

Emergency Operating Procedures

E0P

-

Emergency Preparedness

EP

-

Electric Power Research Institute

L

EPRI.

-

Environmental Qualification

EQ

-

' Essential Raw Cooling Water

ERCW

-

Flow Transmitter

FT

-

,

General Employee Training

GET.

-

Generic Letter

GL

-

Health Physics

HP

-

Integrated Design Inspection

IDI

-

Institute for Nuclear Power Operations

INP0

-

Inspection Report..

IR-

-

Independent Safety Engineering Group

ISEG

-

Inservice Inspection

ISI.

-

' Inservice Testing

IST

-

Liraiting Cordition'for Operation

LC0

-

Licensee Event Report

.LER

-

Microbiologically Incuced Corrosien

'MIC

-

MILES

-

Multiple Integrated Laser Engagen.ent System

Motor Operated Valve Actuators

MOVAT

-

Main Steam Isolation Valve

MSIV

-

NMRG

-

Nuclear Maintenance Review Group

Notice of Unusual Event

NOUE

-

Nuclear Regulatory Commissior..

NRC

-

Nuclear Reactor Regulation

.NRR

-

Nuclear Safety Review Board

NSRB

-

Over Power Delta Temperature

OPDT

-

Office of Special Projects

OSP

-

Over Temperature Delta Temperature

OTDT

-

Preventive Maintenance

PM

-

Post Modification Testing

PMT

-

Plant Operations Review Ccmaittee

PORC

-

Pressurized Water Reactor

PWR

-

Quality Assurance

QA

-

Q6alified Maintenance Document System

QMDS

-

Ouality Verification Inspection

QVI

-

Region II

RII

-

Radiation Centrolled Area

RCA

-

Reactor Coolant System

RCS

-

RHR

Residual Heat Removal

-

Replacement Items Program

RIP

-

. _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ - - _ _ _ - _ _ _ _ _ - - _ _ _ _ _ _ _ - _ _ _ _ _ _ _ _ _ _ _ -

( ,.

.

_

_

- _ _ _ _ _ _ _ _ .

_ _ _ -

. - _ .

_______ _

ff jr , y

'

4j

.c

66;

'

,

Resistance Temperature Device

RTD-

--

Systematic Assessment of Licensee Performance

SALP.:

-

Steam Generators Owners Group

SG0G-

-

Surveillance Instruction

SI'

--

Sequoyah Nuclear Performance Plan

SNPP

-

.

System Operating Instruction-

. 501

.

' Temporary Alterations

' TACFs

.

-

Turbine Driven Auxiliary Feedwater Pump

' TDAFW-

-

Technical Specifications

TS

.

Technical Specification Change Request

TSCR

-

Tennessee Valley Authority

TVA'

-

TVAPD

'TVA Projects Division (NRC)

-

Upper Head Injection

UHI

-

Volume' Control Tank

VCT-

-

.

I

L

-

a

,

,

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