ML20195E585: Difference between revisions

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{{#Wiki_filter:_ _ _ _ - _ _ _ _ _ _ _ _ _ _ _
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Q             Indian Point 3
Q Indian Point 3
                                        ~
~
Nuclear Powie Plant PO. Box 215
Nuclear Powie Plant PO. Box 215 v A 10511 e
  "    e      Buchanan New voA 10511 914 739 8700
Buchanan New o
      #> NewYorkPower 4# Authority May 21, 1986 IP3-WAJ-027Z IP3-JAS-026B Docket No. 50-286 License No. DPR-64 Dr. Thomas E. Murley Regional Administrator Region I U.S. Nuclear Regulatory Commission 631 Park Avenue King of Prussia, PA 19406
914 739 8700
#> NewYorkPower 4# Authority May 21, 1986 IP3-WAJ-027Z IP3-JAS-026B Docket No. 50-286 License No. DPR-64 Dr. Thomas E. Murley Regional Administrator Region I U.S. Nuclear Regulatory Commission 631 Park Avenue King of Prussia, PA 19406


==SUBJECT:==
==SUBJECT:==
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==Dear Dr. Murley:==
==Dear Dr. Murley:==
 
The mid-cycle steam generator tube inspection committed to by the Authority during the August 20, 1985 meeting with the NRC staff has been completed.
The mid-cycle steam generator tube inspection committed to by the Authority during the August 20, 1985 meeting with the NRC staff has been completed. As agreed upon at the August meeting the mid-cycle inspection consisted of an inspection of 100% of the hot leg tubes up to the second support plate.
As agreed upon at the August meeting the mid-cycle inspection consisted of an inspection of 100% of the hot leg tubes up to the second support plate.
Attachment I to this letter summarizes the results of this inspection. This report is provided in accordance with Section 4.9.C of the Indian Point 3 Technical Specifications.
Attachment I to this letter summarizes the results of this inspection. This report is provided in accordance with Section 4.9.C of the Indian Point 3 Technical Specifications.
Based on the final inspection results, Steam Generator 31 was classified as Category C-3 (1% of the tubes inspected defective) as defined in Technical
Based on the final inspection results, Steam Generator 31 was classified as Category C-3 (1% of the tubes inspected defective) as defined in Technical Specification Table 4.9-1.
                                                                        ~~
~~
Specification Table 4.9-1.
All defective tubes identified by the inspection were plugged.
All defective tubes identified by the inspection were plugged.
The Authority will submit a written follow-up of this report in accordance with Technical Specifications. Included will be a review of the operating chemistry for the period since the last refueling outage. This status report was committed to by the Authority at the August 20 meeting.
The Authority will submit a written follow-up of this report in accordance with Technical Specifications. Included will be a review of the operating chemistry for the period since the last refueling outage. This status report was committed to by the Authority at the August 20 meeting.
Sincerely,          ,
Sincerely,
        ,        [ 'UM W   iam A. Jos ger                                                     - "
[ 'UM W
esident ana er                                             r f
iam A. Jos ger esident ana er r
WAJ:JAS: ad
f WAJ:JAS: ad 3
      \                                                                 3 M esident Inspectors' Office                                     8 l
\\M esident Inspectors' Office 8 l 8606090145 860521 PDR ADOCK 05000286 G
8606090145 860521 PDR     ADOCK 05000286 G                 PDR
PDR


ATTACHMEtiT I STEAM                     NUMBER OF                     NUMBER OF GENERATOR                 TUBES INSPECTED               PLUGS INSTALLED 31                         2690                           27 32                         2913                           20 33                         2941                           21 34                         2963                           27 Inspection consisted of 100% of the hot leg tubes up to the second support plate.
ATTACHMEtiT I STEAM NUMBER OF NUMBER OF GENERATOR TUBES INSPECTED PLUGS INSTALLED 31 2690 27 32 2913 20 33 2941 21 34 2963 27 Inspection consisted of 100% of the hot leg tubes up to the second support plate.
                                                                                              %}}
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Latest revision as of 18:52, 10 December 2024

Forwards Results of mid-cycle Insp of Steam Generators,Per 850820 Commitment.Steam Generator 31 Classified as Category C-3,per Tech Spec Table 4.9-1.All Defective Tubes Plugged
ML20195E585
Person / Time
Site: Indian Point Entergy icon.png
Issue date: 05/21/1986
From: Josiger W, Josigner W
POWER AUTHORITY OF THE STATE OF NEW YORK (NEW YORK
To: Murley T, Uurley T
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
References
IP3-JAS-026B, IP3-JAS-26B, IP3-WAJ-027Z, IP3-WAJ-272, IP3-WAJ-27Z, NUDOCS 8606090145
Download: ML20195E585 (2)


Text

_ _ _ _ - _ _ _ _ _ _ _ _ _ _ _

Q Indian Point 3

~

Nuclear Powie Plant PO. Box 215 v A 10511 e

Buchanan New o

914 739 8700

  1. > NewYorkPower 4# Authority May 21, 1986 IP3-WAJ-027Z IP3-JAS-026B Docket No. 50-286 License No. DPR-64 Dr. Thomas E. Murley Regional Administrator Region I U.S. Nuclear Regulatory Commission 631 Park Avenue King of Prussia, PA 19406

SUBJECT:

Indian Point 3 Nuclear Power Plant, Mid-Cycle Inspection of Steam Generators

Dear Dr. Murley:

The mid-cycle steam generator tube inspection committed to by the Authority during the August 20, 1985 meeting with the NRC staff has been completed.

As agreed upon at the August meeting the mid-cycle inspection consisted of an inspection of 100% of the hot leg tubes up to the second support plate.

Attachment I to this letter summarizes the results of this inspection. This report is provided in accordance with Section 4.9.C of the Indian Point 3 Technical Specifications.

Based on the final inspection results, Steam Generator 31 was classified as Category C-3 (1% of the tubes inspected defective) as defined in Technical Specification Table 4.9-1.

~~

All defective tubes identified by the inspection were plugged.

The Authority will submit a written follow-up of this report in accordance with Technical Specifications. Included will be a review of the operating chemistry for the period since the last refueling outage. This status report was committed to by the Authority at the August 20 meeting.

Sincerely,

[ 'UM W

iam A. Jos ger esident ana er r

f WAJ:JAS: ad 3

\\M esident Inspectors' Office 8 l 8606090145 860521 PDR ADOCK 05000286 G

PDR

ATTACHMEtiT I STEAM NUMBER OF NUMBER OF GENERATOR TUBES INSPECTED PLUGS INSTALLED 31 2690 27 32 2913 20 33 2941 21 34 2963 27 Inspection consisted of 100% of the hot leg tubes up to the second support plate.

%