ML20127G554: Difference between revisions

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                                                                                          .Y NOMTNEMN                         STATES                 POWER         COMPANY Monticello, Minnesota 55362 January 18, 1973 Ur. Boyce H. Grior, Director Olroctorate of Requietory Operations Rogion 111 United States Atomic Ener6y Coma.ission 799 Boosevelt Road Glen Ellyn, Illinois                   61037 Doar Mr. Grier:
.Y NOMTNEMN STATES POWER COMPANY Monticello, Minnesota 55362 January 18, 1973 Ur. Boyce H. Grior, Director Olroctorate of Requietory Operations Rogion 111 United States Atomic Ener6y Coma.ission 799 Boosevelt Road Glen Ellyn, Illinois 61037 Doar Mr. Grier:
                                                        .'.ONrtCELLO (UCLE A R GENERAfim PLANT Docket. (b. 50-263 Licenso No. DPR-22                                                           ,
.'.ONrtCELLO (UCLE R GENERAfim PLANT A
Throo containment icolation valves at the %nticolio.fbclear Generating Plant have boon found to lcak in excess of the Technical Specification limit. These butterfly valvos used ;n the containnunt vent, valves purgo, andare torus-to-reactor offset dick, T-ring,lding     bui      vacuum brnakor systems.           Tho leakage rate of two of these valvos has been reduced to within the specified limit by adjusteent of the valvo operating linkage. Repair of the third valve is in progress. :n each case, a second isolation valve in the same line was found to have acceptable lookogo. Invostigation of the cause of the leakage problona is in progress.
Docket. (b. 50-263 Licenso No. DPR-22 Throo containment icolation valves at the %nticolio.fbclear Generating Plant have boon found to lcak in excess of the Technical Specification limit. These butterfly valvos used ;n the containnunt vent, valves are offset dick, T-ring,lding vacuum brnakor systems.Tho leakage rate purgo, and torus-to-reactor bui of two of these valvos has been reduced to within the specified limit by adjusteent of the valvo operating linkage. Repair of the third valve is in progress.
:n each case, a second isolation valve in the same line was found to have acceptable lookogo.
Invostigation of the cause of the leakage problona is in progress.
Yours very truly, C E Larson Plant Manager t0RTHERN STATES' F0flER COIPAf#
Yours very truly, C E Larson Plant Manager t0RTHERN STATES' F0flER COIPAf#
CEt/kik cc: File                                     .
CEt/kik cc: File
                                                                                                                                                  /
/
                                                          ~
9211170374 730118
9211170374 730118                                                                               %"g/f a f;y 7               s ..' y" Y
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              .#   j~ ,                        OlVISION OF COMPLI ANCE 3                                               REGION lli                                             I disijg e                                 799 ROOSEVELT ROAD GLEN ELLYN, ILLINols 60137                               ,,
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i A. RO Inspection Report No.                                                                 I r
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Transmittal Date         :                                                               !
OlVISION OF COMPLI ANCE 3
Distribution:                                  Distribution:
REGION lli I
RO Chie f, FS&EB                               R0 Chie f, FS&"3 RO:HQ (5)                                       RO: liq (4)
disijg e 799 ROOSEVELT ROAD GLEN ELLYN, ILLINols 60137 (sta)ess 2sso i
DR Central Files                               L:D/D for Fuel & Materials Regulatory Standards (3)                       DR Central Files Licensing (13)
A.
B.     RO Inquiry Report No.
RO Inspection Report No.
Transmittal Date     :
I r
Distribution:                                  Distribution:
Transmittal Date Distribution:
4 RO Chie f, FS&EB                               R0 Chie f, FS&EB RO:HQ (5)                                     RO:HQ DR Central Files                               DR Central Files Regulatory Standards (3)
Distribution:
RO Chie f, FS&EB R0 Chie f, FS&"3 RO:HQ (5)
RO: liq (4)
DR Central Files L:D/D for Fuel & Materials Regulatory Standards (3)
DR Central Files Licensing (13)
B.
RO Inquiry Report No.
Transmittal Date Distribution:
Distribution:
RO Chie f, FS&EB R0 Chie f, FS&EB 4
RO:HQ (5)
RO:HQ DR Central Files DR Central Files Regulatory Standards (3)
Licensing (13)
Licensing (13)
C. Incident Notification From: Northern Statee Power Co. 50-263 (Licensee & Docket No. (or License No.)
C.
Transmittal Date             -
Incident Notification From: Northern Statee Power Co.
May 29, 1973 Distribution:                                   Distribution:
50-263 (Licensee & Docket No. (or License No.)
R0 Chie f , F5 EB                               R0 Chie f, FS&EB RO:HQ (4)                                       RO:HQ (4)
Transmittal Date May 29, 1973 Distribution:
Distribution:
R0 Chie f, F5 EB R0 Chie f, FS&EB RO:HQ (4)
RO:HQ (4)
Licensing (4)
Licensing (4)
* L:D/D for Fuel & Materials DR Central tuyg                                 DR Central Files i
L:D/D for Fuel & Materials DR Central tuyg DR Central Files i
                                                                                        -      ..c}}
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Latest revision as of 16:31, 12 December 2024

Ro:Three Containment Isolation Valves Found to Have Leak in Excess of TS Limit.Leakage Rate of Two Valves Reduced to within Specified Limit.Repair of Third Valve in Progress
ML20127G554
Person / Time
Site: Monticello Xcel Energy icon.png
Issue date: 01/18/1973
From: Larson C
NORTHERN STATES POWER CO.
To: Grier B
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION III)
References
NUDOCS 9211170374
Download: ML20127G554 (2)


Text

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.Y NOMTNEMN STATES POWER COMPANY Monticello, Minnesota 55362 January 18, 1973 Ur. Boyce H. Grior, Director Olroctorate of Requietory Operations Rogion 111 United States Atomic Ener6y Coma.ission 799 Boosevelt Road Glen Ellyn, Illinois 61037 Doar Mr. Grier:

.'.ONrtCELLO (UCLE R GENERAfim PLANT A

Docket. (b. 50-263 Licenso No. DPR-22 Throo containment icolation valves at the %nticolio.fbclear Generating Plant have boon found to lcak in excess of the Technical Specification limit. These butterfly valvos used ;n the containnunt vent, valves are offset dick, T-ring,lding vacuum brnakor systems.Tho leakage rate purgo, and torus-to-reactor bui of two of these valvos has been reduced to within the specified limit by adjusteent of the valvo operating linkage. Repair of the third valve is in progress.

n each case, a second isolation valve in the same line was found to have acceptable lookogo.

Invostigation of the cause of the leakage problona is in progress.

Yours very truly, C E Larson Plant Manager t0RTHERN STATES' F0flER COIPAf#

CEt/kik cc: File

/

9211170374 730118

%"g/f a f;y 7 s..' y"

~

Y PDR ADOCK 05000263

/.,/g. 73 Agu h - \\,.

S-PDR

~

gel 88 teg I

,/'

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UNITED STATCS j. 7.'

'. I ATOMIC ENERGY COMMISSION

.# j ~

OlVISION OF COMPLI ANCE 3

REGION lli I

disijg e 799 ROOSEVELT ROAD GLEN ELLYN, ILLINols 60137 (sta)ess 2sso i

A.

RO Inspection Report No.

I r

Transmittal Date Distribution:

Distribution:

RO Chie f, FS&EB R0 Chie f, FS&"3 RO:HQ (5)

RO: liq (4)

DR Central Files L:D/D for Fuel & Materials Regulatory Standards (3)

DR Central Files Licensing (13)

B.

RO Inquiry Report No.

Transmittal Date Distribution:

Distribution:

RO Chie f, FS&EB R0 Chie f, FS&EB 4

RO:HQ (5)

RO:HQ DR Central Files DR Central Files Regulatory Standards (3)

Licensing (13)

C.

Incident Notification From: Northern Statee Power Co.

50-263 (Licensee & Docket No. (or License No.)

Transmittal Date May 29, 1973 Distribution:

Distribution:

R0 Chie f, F5 EB R0 Chie f, FS&EB RO:HQ (4)

RO:HQ (4)

Licensing (4)

L:D/D for Fuel & Materials DR Central tuyg DR Central Files i

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