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{{Adams | |||
| number = ML20133P911 | |||
| issue date = 10/24/1985 | |||
| title = Insp Rept 50-278/85-35 on 850930-1004.No Violation or Deviation Noted.Major Areas Inspected:Local Leak Rate Test Program & Containment Integrated Leak Rate Test Procedure | |||
| author name = Golla J, Johnson J, Kucharski S | |||
| author affiliation = NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I) | |||
| addressee name = | |||
| addressee affiliation = | |||
| docket = 05000278 | |||
| license number = | |||
| contact person = | |||
| document report number = 50-278-85-35, NUDOCS 8511010259 | |||
| package number = ML20133P897 | |||
| document type = INSPECTION REPORT, NRC-GENERATED, INSPECTION REPORT, UTILITY, TEXT-INSPECTION & AUDIT & I&E CIRCULARS | |||
| page count = 5 | |||
}} | |||
See also: [[see also::IR 05000930/2010004]] | |||
=Text= | |||
{{#Wiki_filter:_ | |||
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U.S. NUCLEAR REGULATORY COMMISSION | |||
REGION I | |||
Report No. 50-278/85-35 | |||
. Docket No. 50-278 | |||
License No. DPR-56 | |||
Licensee: Philadelphia Electric Company | |||
2301 Market Street | |||
Philadelphia, Pennsylvania 19101 | |||
Facility Name: Peach Bottom Atomic Power Station, Unit 3 | |||
Inspection At: Delta, Pennsylvania | |||
Inspection Co'nducted: September 30 - October 4, 1985 | |||
Inspectors: ** /0/A'// 6 | |||
S. D. Kucharski, Reactor Engineer 'date~ | |||
DsAse; a - n+ u- | |||
. Gefila, ReactoV Engineer date | |||
Approved by: ( / lbYM | |||
J." JohnsonY Chief, Operational date | |||
Programs Section, 08, DRS | |||
l Inspection Summary: | |||
L | |||
Inspection on September 30 - October 4, 1985 (Inspection No. 50-278/85-35) | |||
Areas Inspected: Routine, unannounced inspection of the Local Leak Rate Test | |||
(LLRT) Program and Containment Integrated Leak Rate Test (CILRT) Procedure. | |||
The inspection involved 72 hours onsite by two region-based inspectors. | |||
Results: No violations or deviations were identified. | |||
fM1010259851028 | |||
G ADOCK 05000278 | |||
PDR | |||
: 1 | |||
' | |||
l | |||
. .. | |||
., | |||
DETAILS | |||
1.0 Persons Contacted | |||
Philadelphia Electric Company | |||
~C. Campbell, Project Engineer | |||
*G. Dawson, Results Engineer | |||
*A. Donell, Site QC Supervisor. | |||
*R. Fleischmann, Plant Manager | |||
*A. Fulvio, Technical Engineer | |||
"A. Smith, Operations Superintendent | |||
*A. Wasong, Results Engineer | |||
NRC | |||
*T. Johnson, Senior Resident Inspector | |||
*H. Williams, Resident Inspector | |||
*0enotes those present at exit meeting on October 4, 1985. | |||
. | |||
2.0 Licensee Action on Previous NRC Findings | |||
2.1 (0 pen) Inspector Follow-up Item (50-278/86-10-01): Licensee Not | |||
Performing Type B and C Testing Results Comparison to 0.6 La for | |||
As-found Condition During Non-CILRT Outages. | |||
This item dealt with the method of recording the results for type B | |||
and C leakage tests. The method used by the licensee now masks the | |||
running total for the LLRT criteria. The licensee agrees with the | |||
inspectors' concern, but as of this inspection, has not made any | |||
changes. This item will remain open. | |||
3.0 Local Leak Rate Test Program | |||
3.1 Documents Reviewed | |||
- | |||
ST 30.037 LLRT - RCIC Steam Supply, Revision 5, for penetra- | |||
tion No. N-10, Unit 3 | |||
- | |||
ST 30.126 LLRT - Drywell Chilled Water Isolation Valves, | |||
Revision 3, for penetrations N-53 thru N-56, Unit 3 | |||
- | |||
ST 30.127 LLRT - RBCW Drywell Isolation Valves, Revision 2, | |||
for penetrations N-23 and N-24, Unit 3 | |||
- | |||
LLRT instrumentation calibration records for test box Nos. | |||
1, 2, 3, 4 and 5, standard instruments used to calibrate the | |||
test boxes (rotameters and pressure gages) | |||
l | |||
. | |||
.. . | |||
. . | |||
3 | |||
- | |||
LLRT Test Box Calibration Procedure RT 7.0, Revision 5 | |||
- | |||
LLRT results for 63 containment penetrations | |||
- | |||
Technical Specification 4.7.A.f | |||
3.2 Scope of Review | |||
The inspectors reviewed the above listed documents to determine | |||
compliance with the regulatory requirements of 10 CFR 50, Appendix J, | |||
technical specifications and applicable industry standards. The | |||
inspectors held discussions with the licensee regarding the documen- | |||
tation of test results, the repair and retesting following failed | |||
tests, and the relationship of these items to the "as-found" and | |||
"as-left" conditions of the containment. | |||
3.3 LLRT Procedure Review | |||
The inspectors reviewed specific LLRT procedures being used during | |||
the current outage. These procedures were determined to be techni- | |||
cally accurate and in conformance with the regulatory requirements. | |||
The procedural valve lineups and associated instructions were ade- | |||
quate to allow for the proper venting and draining of test boundaries. | |||
No unacceptable conditions were identified. | |||
3.4 LLRT Instrumentation Calibration Records | |||
The inspectors reviewed the calibration records for the pressure | |||
gages and rotameters in the LLRT test boxes. The calibrations were | |||
current. The standards used also had current calibration and were | |||
traceable to the National Bureau of Standards. No unacceptable * | |||
conditions were identified. | |||
3.5 LLRT Test Box Calibration | |||
The inspectors witnessed the calibration of two local leak rate test | |||
boxes. The test personnel were familiar with the test equipment and | |||
the use of the procedure. The calibration was conducted in accord- | |||
ance with an approved procedure (RT 7.0, Revision 5). The inspectors | |||
verified the documentation of the test result. No unacceptable | |||
conditions were identified. | |||
3.6 LLRT Test Results Evaluation | |||
The inspectors reviewed individual LLRT results and the running | |||
leakage total. The inspectors also discussed analysis of the test | |||
results and the status of repairs and retests with the licensee. | |||
All "as-found" and "as-left" local leak rates are individually item- | |||
ized and incorporated into two running totals, one "as-found" and | |||
one "as-left." This documentation method is being used for CILRT | |||
only. During non-CILRT outages, the licensee uses a different method | |||
__ | |||
. | |||
s: , | |||
:/. | |||
4 | |||
, | |||
of recording LLRT results.. (See paragraph 2.1) No unacceptable | |||
conditions were identified. | |||
.4.0 . Containment Integrated Leak Rate Test (CILRT) | |||
4.1 Documents Reviewed | |||
- | |||
Surveillance Test Procedure ST-12.5-1,. Revision 5, Integrated | |||
Leak Rate Tes' draft version | |||
- | |||
Technical Spe..fications 4.7.A.c, 4.7.A.d | |||
- | |||
FSAR Section 5.2.5.1, Primary Containment Integrity and | |||
Leaktightness | |||
- | |||
Instrument Selection Guide (ISG) Calculation | |||
- | |||
CILRT Volume Fraction Calculation | |||
4.2 Scope of Review | |||
The inspectors reviewed the above listed documents for technical | |||
adequacy and to determine compliance with requirements of technical | |||
specifications,10 CFR 50, Appendix J, and applicable industry | |||
standards. | |||
4.3 Procedure Review | |||
ILRT Procedure ST-12.5-1, Revision 5, was reviewed in its present | |||
draft stage. The final version is also planned to be reviewed by | |||
the inspectors prior to the upcoming ILRT. | |||
4.4 CILRT Instrumentation | |||
The inspectors reviewed the ISG calculation. It was.found to be | |||
appropriate only for the case where all instrumentation is operable | |||
for the duration of the test. 'It is possible to have one or more | |||
sensors (total pressure, drybulb and dewpoint temperature) fail | |||
during the test. In this case, to meet ISG criteria, the test will | |||
have to be run for a longer duration. The licensee agreed to include | |||
an instrument failure analysis in their calculation. The inspectors | |||
had no further questions at this time. | |||
5.0 QA/QC Involvement in LLRT and CILRT . | |||
LLRT and CILRT activities are monitored by plant QC personnel. QC selects | |||
a sample of LLRT's to be monitored from the outage schedule. These LLRT's | |||
are then reviewed in accordance with a " Detailed Monitoring Checklist" | |||
(DMC) which is' specific to the type of test being performed. The CILRT is | |||
also monitored with a DMC which is specific to the CILRT procedures. The | |||
DMC's were found to be comprehensive and technically useful from a QA/QC | |||
. | |||
. , . , | |||
. | |||
;. | |||
5 | |||
standpoint. QC personnel were knowledgeable of their responsibilities. | |||
No unacceptable ~ conditions were identified. | |||
6.0 Facility Tours | |||
The inspectors made several tours of the facility including the control | |||
room, turbine floor and secondary containment. General housekeeping of | |||
the facility was good. No unacceptable conditions were identified. | |||
7.0 Exit-Meeting | |||
A meeting was held on October 4, 1985, to discuss the scope and findings | |||
of the inspection as described in this report (see Section 1 for | |||
attendees). At no time during the inspection were written inspection | |||
findings provided to the licensee. | |||
/ | |||
}} | |||
Revision as of 22:53, 22 July 2020
| ML20133P911 | |
| Person / Time | |
|---|---|
| Site: | Peach Bottom |
| Issue date: | 10/24/1985 |
| From: | Joe Golla, Jerrica Johnson, Kucharski S NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I) |
| To: | |
| Shared Package | |
| ML20133P897 | List: |
| References | |
| 50-278-85-35, NUDOCS 8511010259 | |
| Download: ML20133P911 (5) | |
See also: IR 05000930/2010004
Text
_
_
, __
, .
.
~ .
U.S. NUCLEAR REGULATORY COMMISSION
REGION I
Report No. 50-278/85-35
. Docket No. 50-278
License No. DPR-56
Licensee: Philadelphia Electric Company
2301 Market Street
Philadelphia, Pennsylvania 19101
Facility Name: Peach Bottom Atomic Power Station, Unit 3
Inspection At: Delta, Pennsylvania
Inspection Co'nducted: September 30 - October 4, 1985
Inspectors: ** /0/A'// 6
S. D. Kucharski, Reactor Engineer 'date~
DsAse; a - n+ u-
. Gefila, ReactoV Engineer date
Approved by: ( / lbYM
J." JohnsonY Chief, Operational date
Programs Section, 08, DRS
l Inspection Summary:
L
Inspection on September 30 - October 4, 1985 (Inspection No. 50-278/85-35)
Areas Inspected: Routine, unannounced inspection of the Local Leak Rate Test
(LLRT) Program and Containment Integrated Leak Rate Test (CILRT) Procedure.
The inspection involved 72 hours8.333333e-4 days <br />0.02 hours <br />1.190476e-4 weeks <br />2.7396e-5 months <br /> onsite by two region-based inspectors.
Results: No violations or deviations were identified.
fM1010259851028
G ADOCK 05000278
- 1
'
l
. ..
.,
DETAILS
1.0 Persons Contacted
Philadelphia Electric Company
~C. Campbell, Project Engineer
- G. Dawson, Results Engineer
- A. Donell, Site QC Supervisor.
- R. Fleischmann, Plant Manager
- A. Fulvio, Technical Engineer
"A. Smith, Operations Superintendent
- A. Wasong, Results Engineer
NRC
- T. Johnson, Senior Resident Inspector
- H. Williams, Resident Inspector
- 0enotes those present at exit meeting on October 4, 1985.
.
2.0 Licensee Action on Previous NRC Findings
2.1 (0 pen) Inspector Follow-up Item (50-278/86-10-01): Licensee Not
Performing Type B and C Testing Results Comparison to 0.6 La for
As-found Condition During Non-CILRT Outages.
This item dealt with the method of recording the results for type B
and C leakage tests. The method used by the licensee now masks the
running total for the LLRT criteria. The licensee agrees with the
inspectors' concern, but as of this inspection, has not made any
changes. This item will remain open.
3.0 Local Leak Rate Test Program
3.1 Documents Reviewed
-
ST 30.037 LLRT - RCIC Steam Supply, Revision 5, for penetra-
tion No. N-10, Unit 3
-
ST 30.126 LLRT - Drywell Chilled Water Isolation Valves,
Revision 3, for penetrations N-53 thru N-56, Unit 3
-
ST 30.127 LLRT - RBCW Drywell Isolation Valves, Revision 2,
for penetrations N-23 and N-24, Unit 3
-
LLRT instrumentation calibration records for test box Nos.
1, 2, 3, 4 and 5, standard instruments used to calibrate the
test boxes (rotameters and pressure gages)
l
.
.. .
. .
3
-
LLRT Test Box Calibration Procedure RT 7.0, Revision 5
-
LLRT results for 63 containment penetrations
-
Technical Specification 4.7.A.f
3.2 Scope of Review
The inspectors reviewed the above listed documents to determine
compliance with the regulatory requirements of 10 CFR 50, Appendix J,
technical specifications and applicable industry standards. The
inspectors held discussions with the licensee regarding the documen-
tation of test results, the repair and retesting following failed
tests, and the relationship of these items to the "as-found" and
"as-left" conditions of the containment.
3.3 LLRT Procedure Review
The inspectors reviewed specific LLRT procedures being used during
the current outage. These procedures were determined to be techni-
cally accurate and in conformance with the regulatory requirements.
The procedural valve lineups and associated instructions were ade-
quate to allow for the proper venting and draining of test boundaries.
No unacceptable conditions were identified.
3.4 LLRT Instrumentation Calibration Records
The inspectors reviewed the calibration records for the pressure
gages and rotameters in the LLRT test boxes. The calibrations were
current. The standards used also had current calibration and were
traceable to the National Bureau of Standards. No unacceptable *
conditions were identified.
The inspectors witnessed the calibration of two local leak rate test
boxes. The test personnel were familiar with the test equipment and
the use of the procedure. The calibration was conducted in accord-
ance with an approved procedure (RT 7.0, Revision 5). The inspectors
verified the documentation of the test result. No unacceptable
conditions were identified.
3.6 LLRT Test Results Evaluation
The inspectors reviewed individual LLRT results and the running
leakage total. The inspectors also discussed analysis of the test
results and the status of repairs and retests with the licensee.
All "as-found" and "as-left" local leak rates are individually item-
ized and incorporated into two running totals, one "as-found" and
one "as-left." This documentation method is being used for CILRT
only. During non-CILRT outages, the licensee uses a different method
__
.
s: ,
- /.
4
,
of recording LLRT results.. (See paragraph 2.1) No unacceptable
conditions were identified.
.4.0 . Containment Integrated Leak Rate Test (CILRT)
4.1 Documents Reviewed
-
Surveillance Test Procedure ST-12.5-1,. Revision 5, Integrated
Leak Rate Tes' draft version
-
Technical Spe..fications 4.7.A.c, 4.7.A.d
-
FSAR Section 5.2.5.1, Primary Containment Integrity and
Leaktightness
-
Instrument Selection Guide (ISG) Calculation
-
CILRT Volume Fraction Calculation
4.2 Scope of Review
The inspectors reviewed the above listed documents for technical
adequacy and to determine compliance with requirements of technical
specifications,10 CFR 50, Appendix J, and applicable industry
standards.
4.3 Procedure Review
ILRT Procedure ST-12.5-1, Revision 5, was reviewed in its present
draft stage. The final version is also planned to be reviewed by
the inspectors prior to the upcoming ILRT.
4.4 CILRT Instrumentation
The inspectors reviewed the ISG calculation. It was.found to be
appropriate only for the case where all instrumentation is operable
for the duration of the test. 'It is possible to have one or more
sensors (total pressure, drybulb and dewpoint temperature) fail
during the test. In this case, to meet ISG criteria, the test will
have to be run for a longer duration. The licensee agreed to include
an instrument failure analysis in their calculation. The inspectors
had no further questions at this time.
5.0 QA/QC Involvement in LLRT and CILRT .
LLRT and CILRT activities are monitored by plant QC personnel. QC selects
a sample of LLRT's to be monitored from the outage schedule. These LLRT's
are then reviewed in accordance with a " Detailed Monitoring Checklist"
(DMC) which is' specific to the type of test being performed. The CILRT is
also monitored with a DMC which is specific to the CILRT procedures. The
DMC's were found to be comprehensive and technically useful from a QA/QC
.
. , . ,
.
- .
5
standpoint. QC personnel were knowledgeable of their responsibilities.
No unacceptable ~ conditions were identified.
6.0 Facility Tours
The inspectors made several tours of the facility including the control
room, turbine floor and secondary containment. General housekeeping of
the facility was good. No unacceptable conditions were identified.
7.0 Exit-Meeting
A meeting was held on October 4, 1985, to discuss the scope and findings
of the inspection as described in this report (see Section 1 for
attendees). At no time during the inspection were written inspection
findings provided to the licensee.
/