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                        U.S. NJCLEAR REGULATORY COMMISSION
                                      REGION III
                Docket Nos:        50-10: 50-237: 50-249
                License Nos:-      DPR-2: DPR-19: DPR-25
              .
                Report No:        50-010/96014: 50-237/96014 50-249/96014
                Licensee:          Commonwealth Edison Company
                Facility:          Dresden Nuclear Station Units 1. 2 and 3
l              Location:          Opus West III
,                                  1400 Opus Place - Suite 300
l                                  Downers Grove. IL 60515
,
                Dates:            October 21 through December 6. 1996
                Inspectors:      C. Vanderniet. Senior Resident Inspector
.
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                                  J. Hansen. Resident Inspector
                                  D. Roth. Resident Inspector
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                                  C. Settles. Inspe tor. Illinois Department of
                                  Nuclear Sa ety
                Approved By:
                                  FAI'
                                  P. L. Hiland. Chief
                                  Reactor Projects Branch 1
      9702100277 970204
      PDR  ADOCK 05000010
      G                PDR
 
:  .
  .
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!                                      EXECUTIVE SUMMARY
                          Dresden Nuclear Station Units 1. 2 and 3
              iiRC Inspection Report 50-10/96014: 50-237/96014: 50-249/96014
      This routine resident inspection included aspects of licensee operations.
      maintenance, engineering, and plant support. The report covered a 7-week
      period of resident inspection.
      Doerations
      .    The facility was operated in a safe manner and previously identified
            minor deficiencies were corrected (Section 01.1).
      .    The Unit 3 low pressure heater bay had improved accessibility and
            housekeeping; however, minor material deficiencies were identified by
            the inspectors (Section 01.2).
      .    A manual reactor trip was initiated in response to a loss of the 3B
            reactor recirculation motor generator set. Plant and safety equipment
            functioned as expected (Section 02.1).
      .    Unit 3 emergency diesel generator (EDG) ejected a cylinder test valve
            after a surveillance run. No personnel injuries or significant damage
            resulted and after minor repairs the EDG was returned to service
            (Section 02.2).
      Maintenance
      .    In general, maintenance activities were well controlled: however, two
            work stoppages were issued due to non-safety related parts control and
            contractor work practices (Section M1.1).
                                                                                    l
      .    Significant repair work on the 3B reactor recirculation pump motor was  l
            well executed and managed. Root cause for the motor failure was foreign  !
            material intrusion into the stator windings (Section M2.1).              l
      .    Construction era rag was found inside the Unit 3 high pressure coolant
            injection (HPCI) lube oil cooler waterbox. Tube leaks were repaired and
            the system was restored to service (Section M2.2).
      Enoineerina
      .    The licensee failed to perform post-modification testing on the Unit 2/3
            main control room heating, ventilation and air conditioning (HVAC)
            system. This was an apparent violation (Section E2.1).                  l
      .    An engineer failed to enter vendor technical information into the vendor
            equipment technical information program (VETIP) as required by plant    l
            procedures (Section E4.1).
                                              2
 
    .
  .
      .
            Ins)ector review of two tem)orary alterations identified some problems
            wit 1 implementation and tecinical evaluation (Section E4.2).
                                                                                      ,
                                                                                      l
      Plant Support
                                                                                      l
                                                                                      !
      .
            Computer accounting system failed at the beginning of the plant assembly
            drill causing confusion. A thorough drill critique identified
            deficiencies and corrective actions (Section P4.1).
      .
            Problems were identified with the level indication and switch
            calibration on the Unit 1 diesel-driven fire pump (Section F2.1).        '
                                                                                      1
                                                                                      l
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                                                                                      ,
                                              3
 
  -
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                                      REPORT DETAILS
    Summary of Plant Status
          Unit 2 began the period at a reduced load of about 300 MWe as some
          maintenance activities were concluded. The unit was returned to full
          power on October 22.    On October 27 a 2% power derate was initiated due
          to feedwater flow instrument uncertainty. On November 23 a load drop
          was made to facilitate a drywell entry to add oil to the 2A reactor
          recirculation pump motor. The unit was returned to near full power the
          following day. On November 26 the 2% derate was lifted and the unit
          returned to full power. On November 28. power was reducea for changing
          condensate demineralizes and exercising control rod drives. The unit      :
          began a slow power increase on December 2 and returned to full power on
          December 3.
          Unit 3 commenced this inspection period in coastdown in preparation for
          refueling outage D3R14. On October 26. the 3B motor generator (MG) set
          tripped and after a short period of single loop operations the reactor
          was manually tripped on October 27. and a forced outage commenced.
                                      I. OPERATIONS
    01    Conduct of Operations
    01.1 General Comments (71707)
          Routine day-to-day facility operations were observed by inspectors both
          in the control room and in the field. Main control board walkdowns and
          reviews of various operating logs were also performed. Previous          l
          observations discussed in Inspection Re) ort 50-237/249-96013. dated
          December 31. 1996 regarding minor breacdowns in control room decorum.    l
          3-way communications, and responsiveness to annunciators were not
          observed during this inspection period. Generally, operator performance
          inside the control room continued to be crisp and professional. A
          weakness was noted with operations personnel outside the control room.    1
          specifically, operator knowledge of the Unit 1 diesel-driven fire pump    ;
          day tank level switches (paragraph F2.1).
    01.2 Tour of Low Pressure Heater Bay (Unit 3)
      a.  Insoection Scone (71707)
          The inspectors toured Unit 3 low 3ressure heater bay and observed the
          general material condition houseceeping, and temporary alterations
          installed on heater drain valves.
      b. Observations and Findinos
          Overall the inspectors noted significantly improved housekeeping over
          the past nine months; however, numerous undocumented material
          discrepancies were identified. These discrepancies included valves
                                              4
 
    -
  .
            missing packing gland fasteners. open junction and electrical cable pull
            boxes. and misadjusted piping hangers. After a discussion about general
            conditions, several items were identified to the licensee for
            correction.
            Followup tours of the Unit 3 LP heater bay found that the specific items
            had been addressed and a few additional items had been identified by the
            licensee. One of the additional items identified by the licensee was an
            o)en lighting junction box above one of the room exits. The tag for
            t11s item was attached to a cable tray protective cover through a hole
            where the cover bolt and stud had broken off. Additionally. the cover
            had several loose or broken nuts, however, none of these deficiencies    l
            were identified by the licensee.                                          l
        c. Conclusions
            The significant improvement in the housekeeping of the LP heater bay
            allowed a greater portion of the room to be more easily accessible. The
            reduction in contaminated areas further improved accessibility to the
            room.  However, the identification of material condition problems in
            less traveled areas of the plant continued to be a challenge.
      02    Operational Status of Facilities and Equipment
      02.1 Recirculation Motor-Generator (MG) Set "B" Trio (Unit 3)
                                                                                      1
        a. Insoection Stone (71707)
            On October 26. at 1758 the 3B Recirculation pump tripped due to tri) ping
            of the 3B MG set. Onsite response to this event was performed by t1e
            inspectors, and observation of control room personnel performance during
            the power reduction and manual reactor scram was accomplished.    The
            following operational procedures were reviewed:
            .
                  Dresden Annunciator Procedure (DAN) 903-4 A6. 3B RECIRC M-G SET
                  GEN LOCKOUT.
            .
                  DAN 903-4 A7. 3B RECIRC PP DP LO.
            .      DAN 903-4 08, 3B RECIRC PP LOWER LUBE OIL LVL LO.
            .
                  Dresden Operating Abnormal (DOA) 0202-01. Recirculation Pump Trip
                  One or Both Pumps.
            .
                  Dresden General Procedure (DGP) 02-01. Unit 2 (3) NORMAL UNIT
                  SHUTDOWN
            .      DGP 02-03. REACTOR SCRAM
            .      DGP 03-03. SINGLE RECIRCULATION LOOP OPERATION
        b. Observations and Findinos
l
l          The root cause of the MG set trip was not immediately known and single    1
l          loop operation commenced. The inspectors responded to the site and        i
            monitored the reactor down power and the subsequent manual reactor trip  I
            at 0201 on October 27. After the 3B MG set tripped, the 3A MG set was
            reduced to 60 percent power in accordance with approved procedures and
                                              5
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          the unit was stabilized at about 34 percent power. Power was further
          decreased to 25 percent using recirculation flow and a manual reactor
          trip signal initiated.    Systems responded as expected with the exception
          of rod position indication failures for two rods and two intermediate
          range monitor failures. For the evolutions observed plant operators
          followed all appropriate procedures during the course of the shutdown.
          Control room decorum and 3-way communications were maintained throughout
          the event.
      c.  Conclusion
          The plant response to the loss of a single reactor recirculation pump
          was in accordance with expectations and plant design. The control room
          operators followed procedures and conducted an orderly shutdown.
    02.2 Emergency Diesel Generator (EDG) E.iected a Cylinder Test Valve Durina
          Troubleshootina Run (Unit 3)
      a.  Inspection Scone (71707)
          The inspectors observed a test of the Unit 3 EDG and observed the
          licensee's response to the observed test failure. Field observations,
          system and equipment inspection walkdowns were performed before and
          after the valve ejection occurred.    Additionally, the inspectors
          reviewed the following documentation
                                                                                    l
          .      Vendor Equipment Technical Information Program (VETIP) Manual
                  1163. Electro-Motive Diesel Engine.
          .
                  Dresden Electrical Surveillance (DTS) 6600-01. Diesel Generator
                  Governor Oil Change and Compensation Adjustment
          .      Dresden Operations Surveillance (DOS) 6600-01. " Diesel Generator
                  Surveillance Test."
      b.  Observations and Findinas
          On November 24. the inspectors observed performance of Dresden
          Electrical Surveillance (DTS) 6600-01 for the Unit 3 EDG. No
          abnormalities were noted during the initial performance of the test.
          Subsequent to test performance, the Shift Manager informed the
          inspectors that the EDG had ejected a cylinder test valve from
          Cylinder 20. The High Voltage Operator (HVO) had entered the room to
          secure the EDG and reported that the test valve had blown out. The
          inspectors returned to the Unit 3 EDG room shortly after the EDG was
          secured.
                                                                                    I
          The test valve had blown out of Cylinder 20 on the EDG generator end.
          The valve appeared to have impacted the wall directly adjacent to the
          valve and fallen to the floor. No damage was evident from the valve
          ejection, other than carbon buildup on piping near the cylinder test
          valve port. Inspection of the test valve showed no damage or unusual
          wear. No personnel injuries were reported and the licensee immediately    i
          initiated a prompt investigation into the event.                          )
                                                                                    ,
 
                                --        --  . -      -  .        _            __ _ _ - _.
  -
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l                                                                                                l
l                                                                                                .
l        During additional inspection on November 25. the inspectors noted that
          the Unit 3 EDG cylinder test valves did not appear to be threaded into                i
                                                                                                1
l        the cylinder block as far as the test valves on the Unit 2 or 2/3 EDGs.                1
          This information was conveyed to the licensee's team performing the                    !
          prompt event investigation.
l        The prompt investigation c termined that the test valves had been                      j
          replaced in December 1995, and that the ejected valve must have had a                  ,
          relaxed torque that was further loosened due to normal EDG vibrations.                '
          Additionally. Cylinder 20 on the Unit 3 EDG was the cylinder with the
          highest compression pressure on the engine. The licensee did not
          perform a formal root cause evaluation of this event although several
          corrective actions were performed. The EDG was repaired and was                        i
          returned to service on November 27.
      c. Conclusions
          Operations personnel performed the surveillance testing in accordance
          with the appropriate procedures and were observed closely monitoring EDG
          performance.
    08    Miscellaneous Operations Issues (92700)
    08.1  (Closed) Violation (50-237:249/95010-03): Control of Overtime Not
          Implemented In Accordance With Generic Letter (GL) 82-12. Revision 1 to
          Dresden Operating Procedure 01-09. Control of Overtime authorized
          November 14, 1995, incorporated the guidance established in GL 82-12.
          This action appeared adequate to prevent recurrence: however, the
          recently completed independent safety inspection (ref. IR 50-237:249/96-
          201, dated December 24, 1996. Section 6.3.3) identified continuing
          problems with corrective action for control of overtime. This item is
          closed and further followup will be documented against Independent
          Safety Inspection (ISI) Deficiency 50-237:249/96-201-29
    08.2 (Closed) Insoector Followuo item (IFI) 50-237:249/96002-04:    Atmospheric
          Containment Atmosphere Dilution (ACAD) Operating and Surveillance
          Procedures' Bands Differ. The inspectors noted that the ACAD system air
          receiver operating pressure band was being maintained at 44 to 57 psig,
          which was above the band in Dresden Operating Procedure (DOP) 2500-01.
          "ACAD Dilution Subsystem Operation" (41 to 52 psig). Dresden Operating
          Surveillance (DOS) 2500-01. "ACAD Compressor Surveillance," and Dresden
          Administrative Technical Requirements (DATR) both listed a pressure band
          of 44 to 57 psig. To resolve this issue, the licensee planned to revise
          the appropriate ACAD procedures. The inspector reviewed the revised
          ACAD procedure (DOP 2500-01) and the changes to the UFSAR and had no
          further concerns. This item is closed.
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                                        II. Maintenance
                                                                                      1
      M1    Conduct of Haintenance                                                    l
                                                                                      1
,
      M1.1 General Comments (62707)
'
            In general, maintenance activities at the facility were well controlled  1
                                                                                      l
            and performed in accordance with approved work packages and procedures.  1
            Numerous tasks were observed in the field and minor observations were    i
            discussed with the appropriate licensee staff. Scheduling and work
            planning continued to be difficult 3roblems. This was evident when a
            stop work order was issued during t1e conduct of maintenance which left
            an oil pump for both the 2A and 2B MG set oil skids out of service,
            thereby leaving both MG sets in a more vulnerable condition.              i
            Significant work activities that were performed during this inspection    .
            period not receiving specific comment included the following;            l
            .      3D Electromatic Relief Valve Flange Leak Repair
            .      Unit 3 EDG Power Pack Replacement
            Additionally, during this report period the licensee issued two stop
            work orders. The first, issued November 21. regarded the retraining of    l
            contractor personnel in the use of nuclear standard work procedures.      i
            This was in response to a failure of contract worker personnel to comply  l
            with facility safe work practices. The second, issued November 24
            regarded the procurement and use of non-safety related parts. This was
            partially in response to the 3A control rod drive pump discharge
            isolation valve that was installed with a through wall pinhole leak.
            Both work stoppages were of short duration and were appropriate
            resomses to address specific maintenance problems.
      H2    Maintenance Material Condition of Facility and Equipment
      M2.1  "B" Reactor Recirculation (RR) Pumo Motor Repair (Unit 3)
        a. Inspection Scope (62707)
            During the report period, the inspectors observed licensee actions to
            troubleshoot and repair the 3B reactor recirculation (RR) motor trip.
            Portions of the field preparation and actual repair were observed by the
            inspectors. In addition, work package preparation and s3ecial rigging
            and load testing documentation were reviewed including t1e following:
            .      Vendor Manual GEK-26132. " Boiling Water Nuclear Reactor
                  Recirculating Water Pump Motors for the Dresden 11 and III nuclear
                  power station of the Commonwealth Edison Company by the General
                  Electric Atomic Power Equipment Department."
            .      Special Procedure (SP) 96-11-019. "3B RR Pump Motor In-place
                  Repair."
,
                                                8
 
  -
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      *      Dresden Engineering Document 5254777. " Reactor Recirculation Pump
              Motor Refurbishment - Details for the Engineered Impact Mat -
              Unit 3."
      .      Dresden Engineering Document 5257492. " Reactor Recirculation Pump
              Motor Refurbishment - Details for Pump Bowl Shimming. Engineered
              Impact Mat and Rigging."
      .      Dresden Engineering Document 5253222. " Rigging of the 3B Recir.
              Pump Motor End Bell. Rotor and Stator to Repair the Motor in
              Place."
    b. Observations and Findinas
      After the October 26, 3B RR pump MG set trip. the licensee's              ,
      troubleshooting effort located a ground in the pump motor. Two            l
      approaches to resolve the problem were developed; repair the motor in-    '
      place, or replacement with a rebuilt motor. A rebuilt motor was
      obtained and brought to the site, but work to repair in-place continued.
      The repair work included load-testing the drywell monorail: design.        l
      testing, and installation of an engineered impact mat: development of a    !
      rigging plan for the motor endbell, rotor and stator; and identifying      j
      possible repair techniques. The plan called for the removal of the        !
      motor endbell and rotor and the lifting of the stator. The stator
      needed to be lifted high enough to allow access for inspection and        !
      repair. Once the package was finally prepared, a special )lant            !
      operations review committee (PORC) reviewed and approved t1e plan.        !
      During the preparation of the work, the inspectors reviewed selected
      portions of the packages and observed monorail and impact mat testing.    j
      The use of a computer-generated animation of the lifting process greatly  1
      aided all personnel in understanding the job. Also, the assignment of
      the Operations Manager as a dedicated project manager ensured continuity
      on the project.
      During the stator inspection a small piece of banding material was
      discovered shorting one motor phase. The foreign material was removed
      and the damaged area of the windings repaired. After successfully
      testing the windings, the motor was reassembled. The piece of banding      ,
      material most likely entered the motor in late 1990 to early 1991 time    l
      frame when the endbell had been removed for maintenance. The banding
      material was similar to material used to secure component identification
      label plates inside the drywell. The licensee suspected that some of
      this material was dropped into the motor and eventually shorted the
      stator. Additional foreign material found inside the motor was removed.
      The intrusion of foreign material into various components at the
      facility has been a longstanding problem. However, the inspectors'
      recent observations of foreign material exclusion (ME) practices
      indicated that significant improvements have been made over past
      practices.
                                          9
 
                                    _
    -
  .
l
          The ins)ectors observed various activities as the work progressed and
          noted tlat the job was well managed and skillfully performed.
          Disassembly, re) air. and reassembly progressed as expected and no major
          problems with t1e work plans were encountered. Radiation protection
          controls and practices were followed and the use of a video monitor for
t          the viewing of the work was a good "as low as reasonably achievable"
l          (ALARA) practice.
      c.  Conclusions
          The 3B RR pump motor repair was well coordinated.      Management and Site
          Quality Verification oversight were maintained and no significant
!          unanticipated problems occurred. The finding of several pieces of
          foreign material inside a major component was not a new issue at the
          facility and efforts to improve FME continued to receive appropriate
          management attention.
      M2.2 Rao Found in Hiah Pressure Coolant Iniection (HPCI) Lube Oil Cooler.
            (Unit 2)
      a.  Inspection Scone (62707)
          The inspectors ins)ected the Unit 2 HPCI lube oil cooler and observed
          the rag found by t1e licensee during emergent maintenance work. A
          review of the licensee's efforts to identify when the rag entered the
          system was also performed,
      b.  Observations and Findinas                                                  !
          The HPCI system was declared inoperable on November 27. due to excessive    l
          water contamination in the turbine lubricating oil. While performing        i
          maintenance to repair the water leaks in the lube oil cooler,
          maintenance personnel discovered a rag in the cooler water box. The rag
          covered a significant portion of the cooler tube openings and appeared
          to have been acting as a filter for the cooling medium.
          The licensee suspects that the rag had been used as an FME cover during
          facility construction and was never removed. The assumption was
          substantiated due to the lack of finding any previous maintenance items
          that required removal of the HPCI lube oil cooler endbells in the
          maintenance database.    Further database searches showed that no recorded
          maintenance work had been performed on the cooler or cooling system that
          would have allowed visual identification of the rag since the system was
          originally placed in service. The licensee also reviewed surveillance
          test data and did not identify any instance of the HPCI system being
          inoperable or degraded due to inadequate lube oil cooler performance.
          Repair efforts were completed and the cooler was reassembled and
          satisfactorily tested.      Unit 2 HPCI was returned to service on
          December 1, with no further problems.
                                              10
 
.____m        . . . _ _      ._. _ _ _ _ _ _ _ . _ _ _ _                          . _ _ _ _ . _ _ _ . _
      -
.    .
0
1
!
            c.      Conclusions
:
i-                  All observed maintenance activities were performed in a skilled manner,
i
                    however, the discovery of the rag in the cooler further emphasized the
i                    need to continue monitoring FME controls.
;
            -
                                                                                                          I
        M8          Miscellaneous Maintenance Issues (92902)                                            I
i        M8.1        (Closed) Insoector Followuo Item 50-237/249-95008-01: Failure to Follow
                    Procedure Resulted in Two Inoperable Core Spray Systems. On April 24,                '
                    1995, the licensee reused o-rings on environmentally qualified equipment            l
}                    and only hand tightened the transmitter covers in violation of the                  l
*
                      3rocedure. The inspectors reviewed information on reused o-rings and                )
.
                      land tightened covers in CHRON # 0308805 and a referenced letter from              '
i                    Rosemount. The information a)peared adequate to support the licensee's
l                    operability determination. T11s item is closed.
a
:
                                                          III. Enaineerina
        E2          Engineering Support of Facilities and Equipment
        E2.1 Failure to Perform Adeouate Post-Modification Testina of the Control
                    Room Heatina and Air Conditionina (HVAC) System (Units 1. 2 and 3)
            a.        Insoection Scope (37551)
                    The inspectors continued to observe and monitor the licensee's progress
                      in correcting control room HVAC design and testing deficiencies. The
                      following documentation was reviewed:
                    .
                            Modifications M12-2/3-82-1. M12-0-87-005 and M12-0-86-006: Unit 1
                            Control Room Modifications.
                      *      DTS 5750-06, " Control Room Standby HVAC Air Filtration Unit, and
                            Refrigeration Condensing Unit Performance Requirements," dated
                            August 24, 1996.
            b.      Observations and Findinas
                    The licensee continued work on sealing penetrations into the Unit 2/3
                    control room, auxiliary computer room, and train "B" HVAC rcom. At the
                      close of this report period, efforts to remove a temporary alteration
                      and return the auxiliary computer roo.n into the control room envelope
                    were unsuccessful. The licensee continued testing and achieved and
                    maintained positive pressure requirements with the exception of the
                      auxiliary computer room. Further work was planned to correct problems
                      in the computer room and return the room to the control room envelope.
                      Background information on this issue can be found in Inspection Report
                      96013 (paragraph E2.4) and Independent Safety Inspection (ISI) Report
                      96-201 (paragraph 4.6.4.1). The significance of this event was
                      previously considered an Unresolved Item (50-237:249/95013-02).
                                                                  11                                      ;
                                                                                                          I
 
  -
.
    c. ISI Report 96-201. dated December 24. 1997. Daragraoh 4.6.4.1
      Sections 6.4.2 and 9.4-3 of the UFSAR described the design basis for the
      control room HVAC system. Section 6.4.2.4 stated that potential adverse
      interactions between the control room emergency zone and adjacent zones
      that may allow the transfer of toxic or radioactive gases into the
      control room were minimized by maintaining the control room at a            ,
      positive pressure of 1/8-inch water gauge (iwg) during emergency            l
      pressurization modes, and with respect to adjacent areas.
      On October 8. 1996, the licensee declared the control room HVAC system
      inoperable because of the inability to maintain the control room at a
      positive pressure during normal operations and at 1/8 iwg with respect
      to the surrounding areas in the emergency mode.    The control room
      ventilation system had not been maintained or properly tested 'o ensure
      that the system operated within its design basis. Modifications had
      been implemented, or partially implemented, which resulted in negative
      pressure within the control room and the inability to pressurize the      l
      control room to 1/8 iwg in the emergency mode. In addition,
      instrumentation that was used to verify the control room pressure was
      positive in the emergency mode had not been calibrated, and had not been
      installed in accordance with the piping and instrumentation diagram.      j
                                                                                  i
      In September 1996, the licensee began reviewirg open modifications for    '
      the control room ventilation system, and subsequently determined that
      several control room modifications, which had not been completed,        i
      contributed to the inability to pressurize the control room as stated in
      the UFSAR.    These incomplete modifications were identified as a result ,
      of the licensee's efforts to close all modifications or approve the as-  I
      built configuration. The specific modifications affecting the control
      room included:
      .
              M12-0-87-005-D provided for the installation of security equipment
              such as bullet resistant plating for walls and ceilings, new east- l
                                                                                3
              west kitchen and locker room area fire and non-fire rated doors.    I
              and the sealing of new and unused wall and floor penetrations.
              Field work was initiated in August 1991 and completed in          j
              January 1992. Post-modification testina was not oerformed.
                                                                                  !
                                                                                l
      .      M12-0-87-005-E provided supply and exhaust ventilation systems for  i
              the new locker room and kitchen areas, new fire dampers in duct
              work penetrating fire walls, control logic for operation of the
              isolation dampers, and an interlock for the exhaust fans from the
              isolation dampers. Field work was started in September 1991 and    l
              completed by June 1993. The oost-modification testina, includina
              loaic testina and emergency oressurization testina to verify
              1/8 iwa was not oerformed.
      .      M12-0-86-006-C provided supply and return side duct silencers,      j
              thermally insulated duct work, and manual volume dampers in the
                                                                                  :
                                          12
                                                                                  i
 
'
    '                                                                              1
  .
                                                                                  j
                                                                                    1
                                                                                    l
                                                                                    l
                shared return duct works. The field work was started in            !
                March 1989 and the documentation closure was completed in          !
                September 1993. Post-modification testina was not comoleted.
        .      M12-0-86-006-D provided for the removal of existing HVAC duct work
                supports inside the Unit 2 and 3 control room, installed            I
                acoustical tile, installed new duct work including hangers and
                safety chains. reworked existing ductwork inside the control room,
                and removed existing butterfly dampers inside the control room.
                The field work was initiated in June 1989 and the work was          l
                determined to be completed in May 1993. Post-modification testina
                was not completed
        .      M12-2/3-82-1 added the HVAC Train B in 1982; however, the NRC's
                ISI team concluded the modification was not adeouately tested.    l
        Surveillance Procedure (DTS) 5750-06. Revision 3. " Control Room Standby
        HVAC Air Filtration Unit, and Refrigeration Condensing Unit Performance
        Requirements." dated August 24, 1996, only required 1/8 iwg positive
        pressure in the control room and did not ensure thst pressure was        .
        greater than 1/8 iwg for the surrounding areas. In addition, the          l
        instrumentation used to verify the control room differential
        pressure (d)) was not calibrated nor verified to be appro)riate for the
        parameters Jeing measured. Specifically, dp Instruments )PI-2-5740-
        31/32 and 36 for the control room and east turbine building had not been
        calibrated. The licensee also identified that the control room
        instrumentation was mislabeled with respect to the areas being sensed
        and, according to '.he drawings, other sensing lines were misrouted or
        were broken.
      d. Conclusions
        The licensee's failure to perform testing of modifications performed to
        Unit 2/3 control room HVAC system, as discussed above and detailed in
        the ISI Irspection Report 96-201, section 4.6.4.1. dated December 24.
        1996, is an Apparent Violation of 10 CFR 50. Appendix B. Criterion XI.
        " Test Controls." (50-237/249-96014-01).
        The apparent violation is being considered for escalated enforcement
        action in accordance with the " General Statement of Policy and Procedure
        for NRC Enforcement Actions" (Enforcement Policy). NUREG-1600.
        Accordingly, no Notice of Violation is presently being issued for this
        inspection finding. The significance of the issue, and short term
        corrective actions were discussed with the licensee in the exit meeting
        for this inspection period on December 19. 1996.
        Before the NRC makes an enforcement decision, the licensee will be
        provided an opportucity to respond to the ap)arent violation at a pre-
        decisional enforcement conference as descri)ed in the cover letter to
        this report.
                                            13
 
  ._    _. _. , _. .            _.__-.._._._.- _ ~ _ _ - . _ . _ _ _ _ . . _ _ _ . . _.                        -
      -
  .
                                                                                                                              1
                                                                                                                                l
          E3        Engineering Procedures and Documentation
            E3.1 Additional Vodated Final Safety Analysis Report (UFSAR) Discreoancies
                  a.  Insoection Scooe (71707)                                                                                :
                      The inspectors used the UFSAR as a technical reference during a review
                      of findings' from a routine drywell tour. A comparison of actual plant
                      configuration was made to the descriptions contained in the UFSAR. Note
                      that other UFSAR discrepancies regarding the control room HVAC system
                      were documented in Section E2.1.
l                b.  Observations and Findinos                                                                                j
l
!                    Prior to performing a Unit 3 drywell routine tour the inspectors
l                    reviewed various UFSAR sections including section 6.1.1.1                                  " Materials
                      Selection and Fabrication." This section stated, "All piping inside
'
                      containment is covered with metallic mirror-type insulation." During
                      the drywell tour the inspectors found this not to be the case as several
i
'
                      other types of insulation were used on piping. The licensee confirmed
                      that the other types of insulation ident1fied by the inspectors were
                      acceptable for use in the drywell. This discrepancy was discussed with
                      the licensee and a change to the UFSAR and a performance improvement
                      form (PIF) were initiated.
                  c.  Conclusion
                      The above example showed that discrepancies between plant configuration
!
                      and the UFSAR still exist. However, the licensee was taking prompt
                      actions to resolve identified discrepancies.
            E4        Engineering Staff Knowledge and Performance
            E4.1 Failure to Uodate Emeraency Diesel Generator (EDG) Vendor Technical
                      Information Manual (Units 2 and 3)
                  a.  Insoection Scooe (37551)
                      While inspecting the licensee's response to a Unit 3 EDG test valve
                      failure (Section 02.2 of this report), the inspectors reviewed the                                        l
                      approved vendor technical manual.                                  The inspectors compared the approved
                      vendor manual to the conditions that existed in the field and conducted-
                      discussions with the system engineer and engineering management. The
                      following administrative procedures were also reviewed;
                      e      Dresden Administrative Procedure (DAP) 02-10. " Control of Vendor
                              Equipment Technical Information," Revision 5.
                      .      Nuclear Engineering Procedure (NEP) 07-04. "VETIP Process
,                            Control," Revision 0.
i
                                                                                                                                !
                                                                                                                                '
                                                                                      14
                                                                                                                                l
    ,          -                                                                _
 
    -
  .
      b.  Observations and Findings                                                    l
            The inspectors noted that the test valves depicted in the manual were
            different from those installed on the EDGs. During discussion with the      :
            licensee, the correct information was found in the system engineer's
            desk. Maintaining vendor supplied technical information in an
            uncontrolled manner was contrary to the licensee's vendor equipment          l
            technical information program (VETIP). Dresden Administrative                !
            Procedure 02-10. Revision 5. Section E.5 required that " Existing,          i
            uncontrolled, and ircoming ETI (Equipment Technical Information) shall
            be reviewed and added to VETIP so that the latest /most applicable          )
            information is available for station use."                                  l
            In addition. NEP 07-04. Section 5.2.1.2. required that "The person
            receiving new vendor manual revision data shall forward the information
            to the VETIP Coordinator attached to the VETIP Authorization Form
            (Exhibit A) or suitable equivalent."
            The licensee initiated a PIF documenting the misplaced vendor data and      ;
            forwarded the information to the VETIP coordinator for inclusion into        !
            the EDG VETIP manual.                                                        ,
                                                                                        l
      c.  Conclusions                                                                  l
                                                                                        !
            Past weaknesses in the VETIP program were previously documented in
            Inspection Report 96006. section M2.1. dated August 22 1996. The            l
            licensee was not successful in assuring the VETIP was hroperly              i
            implemented. Not entering the EDG test valve technical information          l
            change into the VETIP program as required by approved procedures was a
            Violation of Technical Specification 6.2. Procedures and Programs
            (50-237/249-96014-02).                                                      1
      E4.2 Review of Temocrary Alterations Related to the Control Room HVAC Repair      I
            and the 125Vdc and 250Vdc Batteries (Units 2 and 3)
      a.  Insoection Scooe (37551)
            The inspectors reviewed two installed temporary alterations. The review
            included a field walkdown of the alterations and a review of the
            associated documentation and procedures including:
            .      DAP 05-08. " Control of Temporary System Alterations."
            .      Temporary Alteration No. III-53-96. " Isolate HVAC Supply / Return To
                  and From the Aux Computer Room."
            .      Temporary Alteration No. III-33-96. " Supply Temporary Heat to U2
                  125V and 250V DC Battery Rooms."
      b.  Observations and Findinos
            The auxiliary computer room temporary alteration was installed to
            isolate the room from the control room while the control room walls were
i          sealed. The temporary alteration called for three portable air
l
l                                              15
 
                                          -.
                                                  _ _ . . .__.  .
                                                                      .
                                                                          _- .    _ . _ _ _ _
    -
  .
                                                                                              l
                                                                                              :
        conditioning (AC) units to be placed in the room and vented out the
        auxiliary computer room door. During the walkdown, the inspectors noted
        that the door to the room was left open to accommodate the three exhaust
        trunks used to expel heated exhausts from the portable AC units. This
        arrangement essentially countered any benefit received from the AC units
        because of the free exchange of warmer auxiliary electrical room air
;        into the auxiliary computer room.                                                    l
!
        The Unit 2 battery rooms temporary alteration was installed to ensure
        that the proper temperature was maintained in the battery rooms while
        work was in progress on the normal ventilation system. During the
        walkdown, the ins)ectors observed that the alteration had been installed
        as intended and tlat a firewatch was present. Both doors to both
        battery rooms were also open which, although allowed by the temporary
        alteration. seemed unnecessary and even counterproductive to the
        intended design.
        Additionally, the inspectors noted that the battery rooms were about
        81 F. well abon the required tem)erature of 68 F. This observation was
        conveyed to the licensee and the )attery rooms were returned to normal
        and the firewatch secured. Subsequently, room temperature was monitored
        by hourly operator rounds.
        A documentation review showed that the technical evaluation had been
        identified as not safety related. The documented explanation stated
        that the batteries were safety-related, but the room HVAC system was
        not.
        The 125V and 250V batteries were the most risk significant system at the
        facility and were clearly safety-related. The temporary alteration was
        only concerned with maintaining the room temperatures above 68 F to
        assure the batteries were not in a degraded condition. Therefore. the
        installation of the temporary alteration directly affected the two
        station batteries not just the room HVAC.                                            I
      c. Conclusions
        Although the alterations were installed as written, the design
        effectiveness was flawed. This appeared to be the result of an
        ineffective field walkdown of the alteration and a weak review of the
        design implementation. Additionally, the licensee maintained that the
        battery room alteration only affected the battery room HVAC system and              '
        was not safety-related. Further discussions will be needed to resolve
        this issue: therefore this issue will remain an Unresolved Item
          (50-237/249-96014-03).
                                                                                              4
l
l                                            16
 
  ..    ..      .__ _.    _._______                ___._-__ _ _                            .      _ __  _
    -
  .
                                                                                                                j
                                                                                                                '
l
,
      E6    Engineering Organization and Administration                                                      l
                                                                                                                ,
      E6.1 Enaineerina Deoartment Manaaement Chances (37551)
,            A new Site Engineering Manager, Mr. Russell Freeman, was ao)ointed                                1
l            during the report period. Previously. Mr. Freeman was the )resden Plant                          ;
l            Engineering Superintendent.
      E8    Miscellaneous Engineering Issues (92903)
      E8.1 (Closed) Unresolved Item (50-237/249-95015-05):                  Corner Room Steel.                !
              This issue regarded the corrective action for inadequate corner room                              l
l
              structural steel design margins, and was the subject of escalated                                ;
              enforcement and a civil penalty (EA 96-115) on June 13, 1996. This item                          !
              is closed.                                                                                        !
      E8.2 (Closed) Unresolved Item (50-237/249-96013-02): Control Room                                        i
'
              Ventilation System Operability. This issue regarded the licensee's                                I
              corrective actions to resolve inadequate post-modification testing of
              the control room HVAC system. This issue was reviewed and is an example
              of an apparent violation discussed in Section E2.1 of this re) ort.
              Additional followup of this item will be documented against tais reports                          !
,
              assigned tracking number. This item is closed.                                                    !
                                                                                                                t
                                        IV. Plant Suooort
      P4    Staff Knowledge and Performance in EP                                                            '
      P4.1 Performance durina Assembly Drill (Units 1. 2 and 3)
          a. Inspection Scoce (82701)                                                                          ;
              On November 26 the inspectors observed licensee response to an                                    ,
              unannounced site assembly drill. Documents reviewed included Emergency
              Plant Im)lementing Procedures (EPIP) 0400-01, " Plant Assembly and                                i
              Accounta)ility."
          b. Observations and Findings
              The station alarm was sounded at 1230 and the site assembly drill was
              announced on the station public address system. The inspectors
              responded to assigned assembly points and noted that the computerized
              assembly card reading system was not operating. After being manually
              accounted, the inspectors went to other assE.3bly areas to observe
              activities.
l              In the Administrative Building the accounting 3rocess was in disarray.
              The lunchroom and main hallway were filled wit 1 personnel waiting to be
              counted.  Twenty minutes into the drill the licensee initiated a manual
l            accounting of personnel in the Administration Building. This was                                  ,
              accomplished by handing out sheets of paper to management personnel and
                                                                                                                '
'
                                                                                                                '
                                                17
                                    -                      . - . - - - . _ -    -    --      _ _ -      -  _
 
  .
.
          requiring managers to count assigned personnel. At one point a station
          supervisor directed assigned personnel to leave the Administration
          Building and go to a work area. This was followed by similar direction
          from another su)ervisor. The individual in charge of the accountability
          activities in t1e Administration Building halted the exodus and stated
          that the accounting for all groups would be completed in the
          Administration Building.
          The licensee was able to gain control of the accounting process;
          however, the licensee was not able to complete the accounting within the
          allotted time. Station management determined that aerformance during
          the drill was unsuccessful and another drill was scleduled. The
          licensee's critique was thorough and independently addressed all of the
          inspectors' concerns.
      c. Conclusions
          The difficulty the licensee experienced in accounting for the station
          staff manually demonstrated the there had been an over-reliance on the
          computer counting. The licensee's thorough post-drill critique
          correctiy assessed the weakness in performance and established
          appropriate corrective actions.
    F2    Status of Fire Protection Facilities and Equipment
    F2.1 Problems Identified with Diesel-Driven Fire Pumo (Units 1. 2 and 3)
      a. Insoection Scope (64704)
          The inspectors performed walkdowns of the Unit 1 diesel-driven fire pump
          and all associated equipment and held several discussions with licensee
          staff. The following documentation was also reviewed:
          .      DAN 901-2 E-8. "U1 Fire PP Day Tank Lvl Hi."
          .
                Dresden Fire Protection Surveillance (DFPS) 4123-01. " Unit 1
                Diesel Fire Pump Operability."
          .      Schematic Diagram 12E-6580F, " Fire Protection System Diesel Driven
                Fire Pump Intake Structure."
          .      Wiring Diagram 12E-6580G. " Diesel Driven Fire Pump."
      b. Observations and Findinos
          On November 15. the Unit 1 diesel-driven fire pump failed a surveillance
          run. The cause for the failure was the closing of the fuel su) ply
          solenoid valve that occurred when a power lead to the valve vi] rated off
          a terminal. During subsequent walkdowns of the pump and associated
          components. the inspectors questioned if the local fuel oil storage tank
          level float was operating 3roperly. The work execution center (WEC)
          supervisor was contacted a)out the level indicator and stated that the
          indicator was working properly. Upon further investigation, the
          licensee determined that the level float was not operating properly.
                                            18
 
    -
  .
            The installed level float indicated the tank was between 3/4 and 7/8
            full, when the tank was only a little more than half full.
            The inspectors also questioned the low level alarm switch calibrations
            and requested the latest calibration records. The same WEC supervisor
            was contacted and stated that there was a high level alarm but no low
            level alarm on the tank. The inspectors reverified that there was a low
            level switch, a high and a high-high level switch. The licensee then
            determined that the level switches were not in the calibration 3rogram
            and could not find any documentation of the switches being cali) rated.
            The fuel tank local level indicator float was repaired and the level
            switches were calibrated. The solenoid power lead was reterminated and
            the Unit 1 diesel-driven fire pump successfully passed surveillance
            testing and was returned to service.                                    '
          c. Conclusion
            The fire protection system has had numerous problems over the last few
            months and did not appear to be receiving an adequate level of
            attention. The system operation was not fully understood by some
            members of the plant staff.
      F8    Hiscellaneous Fire Protection Issues (92904)
      F8.1  (Closed) IFT 50-237/249-95008-10: Emergency Lighting. During a fire
i
            protection inspection, the ins)ectors identified that several emergency
            lights were dirty, several lig1ts were aimed improperly, and one light
            was blocked by a plant modification. The licensee permanently relocated
            the blocked emergency light to a new location. The affected emergency
.
'
            lights were correctly aimed. Also, a procedure change was completed to
            Dresden Electrical Surveillance (DES) 4153-02. Safe Shutdown Emergency
            Lighting Quarterly Inspection, to ensure that emergency lights' lamps
            would be inspected and cleaned as necessary.    This item is closed.
                                    VI. Manacement Meetinas
;      X1    Exit Meeting Summary
"
            The inspectors 3 resented the inspection results to members of licensee
            management at t1e conclusion of the inspection on December 19. 1996.
            The licensee acknowledged the findings presented.
            The inspectors asked the licensee whether any materials examined during
            the inspection should be considered proprietary. No proprietary
            information was identified.
                                                19
                                                                                    l
 
                                    . . _ . . _ -
    -
  .
                                                                  ;
                                                                  ,
i
                                PARTIAL LIST OF PERSONS CONTACTED !
l
                                                                  !
l      Licensee
                                                                  !
!                                                                -
    ' S. Perry. Vice President. BWR Operations                    !
l      E. Connell. Design Engineering Superintendent              ;
!      T. Foster. Work Control and Outage Manager                1
      R. Freeman. Plant Engineering Superintendent              !
l      J. Heffley. Units 2 and 3 Station Manager                  ,
;      C. Howland. Radiation Protection Manager                    l
      R. Kundalkar. Site Engineering Manager
l
      T. Nauman. Unit 1 Station Manager                          l
      T. O'Connor. Operations Manager                            i
      F. Spangenburg Regulatory Assurance Manager                I
;
      P. Swafford. Unit 2/3 Maintenance Superintendent
      P. Tzomes. Support Services Director                      :
      D. Winchester. Safety Ouality Verification Director        i
                                                                  !
                                                                  l
                                                                  l
                                                                  .
                                                                  I
I
l                                                                  !
l
'
                                                                  :
                                                          20
l
                                                                    l
l                                                . . . .
 
  __ .  -  . .          .    .          . _ ._ _ __.-__ __    _ . . . _ _ . . _ . - _ _ _ . _ . . _ - _ _ _ _ _ . _ _ _ - . _ _
          -
      .
                                                                                                                                    t
                                            INSPECTION PROCEDURES USED
                                                                                                                                    ,
                IP 37551:  On-site Engineering                                                                                    i
                IP 62707:  Maintenance Observations
                IP 64704:  Fire Protection Program
                IP 71707:  Plant Operations
                IP 82701:  Operational Status of the Emergency Preparedness Program
                IP 92901:  Followup - Plant Operations
                IP 92902:  Followup - Maintenance
i                IP 92903:  Followup - Engineering
l                IP 92904:  Followup - Plant Support
l
                                                                                                                                    !
                                                                                                                                    :
                                                                                                                                    1
                                                                                                                                    l
l
1
l
1
!
l
l
l
l
                                                              21
i
l
l
.
 
  _ . - _ -          . - - .  .__ _ - _ . -        -. . - .
              -
            .
                                                                                                  l
                                                                                                  l
                                                ITEMS OPENED AND CLOSED
l                Ooened                                                                          i
i                                                                                                  l
l                50-237/249-96014-01 APPARENT Failure to Perform Post-Modification Testing for
l                                            VIO    Control Room HVAC System (Apparent Violation).
l                50-237/249-96014-02      VIO    Failure to Follow VETIP Procedure for Incoming l
                                                    Vendor Technical Information.                  1
                  50-237/249-96014-03      URI    Battery Room Temporary Alteration.
l
                  Closed
                  50-237:249/95010-03        VIO    Control of Overtime Not Implemented In
                                                    Accordance With Generic Letter (GL) 82-12.
                  50-237/249-95015-05        URI    Corner Room Steel.
                  50-237/249-96013-02        URI    Control Room Ventilation System Operability.
                  50-237/249-95008-01        IFI    Failure to Follow Procedure Resulted in Two
                                                    Inoperable Core Spray Systems.                !
                  50-237/249-95008-10        IFI    Emergency Lighting.
                  50-237:249/96002-04        IFI    Atmospheric Containment Atmosphere Dilution
                                                    (ACAD) Operating and Surveillance Procedures'
                                                    Bands Differ.
                                                                                                  l
                                                                                                  l
                                                                                                  :
                                                                                                  l
                                                              22
                                                                                                  \
                _ _ _          ,_ .
 
    ._  _ _ _        . _ . . _    .                  -- _ _. _ _ _ _ . .    .. _ _. _._- . . .
              -
      o
.
                                                                                                  '
                                                  LIST OF ACRONYM 3 USED
                AC              Air Conditioning
i                ACAD            Atmospheric Containment Atmosphere Dilution
                ALARA          As Low As Reasonably Achievable                                    I
4
                CFR            Code of Federal Regulations                                      !
  .
                CRD            Coritrol Rod Drive                                                I
!                DAN            Dresden Annunciator Procedure
1
                DAP            Dresden Administrative Procedure
4                DATR            Dresden Administrative Technical Requirements
                DES            Dresden Electrical Surveillance
                DFPS            Dresden Fire Protection Surveillance
                DGP            Dresden General Procedure                                          1
2
                DOA            Dresden Operating Abnormal                                        l
;
                DOP            Dresden Operating Procedure
                DOS            Dresden Operations Surveillance
                dP              Differential Procedure
                DTS            Dresden Technical Surveillance
a                EA              Enforcement Action
;                EDG            Emergency Diesel Generator
-
                EPIP            Emergency Plan Implementing Procedures
                ETI            Equipment Technical Information
;                FME            Foreign Material Exclusion
;                GL              Generic Letter
                HPCI            High Pressure Coolant Injection
                HVAC            Heating. Ventilation, and Air Conditioning
"
                HVO            High Voltage Operator
                IFI            Inspector Followup Item
                ISI            Independent Safety Inspection
,
'
                IWG            Inches Water Gage
                LP              Low Pressure
;                MG              Motor Generator
                MMD            Mechanical Maintenance Department
:                MWe            Megawatts Electrical
                NEP            Nuclear Engineering Procedure                                    l
J                NDV            Notice of Violation                                                '
l                PDR            Public Document Room                                              j
;                PIF            Performance Improvement Form
                PORC            Plant Operations Review Committee
;                asig          Pounds Per Square Inch Gauge
l                1R              Reactor Recirculation
l                UFSAR          Updated Final Safety Analysis Report
i                URI            Unresolved Item
;
                VETIP          Vendor Equipment Technical Information Program
                WEC            Work Execution Center
:
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Revision as of 20:23, 22 July 2020

Insp Repts 50-010/96-14,50-237/96-14 & 50-249/96-14 on 961021-1206.Violations Noted.Major Areas Inspected: Operations,Maintenance,Engineering & Plant Support
ML20134G104
Person / Time
Site: Dresden  Constellation icon.png
Issue date: 02/04/1997
From:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION III)
To:
Shared Package
ML20134G097 List:
References
50-010-96-14, 50-10-96-14, 50-237-96-14, 50-249-96-14, NUDOCS 9702100277
Download: ML20134G104 (23)


See also: IR 05000010/1996014

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U.S. NJCLEAR REGULATORY COMMISSION

REGION III

Docket Nos: 50-10: 50-237: 50-249

License Nos:- DPR-2: DPR-19: DPR-25

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Report No: 50-010/96014: 50-237/96014 50-249/96014

Licensee: Commonwealth Edison Company

Facility: Dresden Nuclear Station Units 1. 2 and 3

l Location: Opus West III

, 1400 Opus Place - Suite 300

l Downers Grove. IL 60515

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Dates: October 21 through December 6. 1996

Inspectors: C. Vanderniet. Senior Resident Inspector

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J. Hansen. Resident Inspector

D. Roth. Resident Inspector

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C. Settles. Inspe tor. Illinois Department of

Nuclear Sa ety

Approved By:

FAI'

P. L. Hiland. Chief

Reactor Projects Branch 1

9702100277 970204

PDR ADOCK 05000010

G PDR

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! EXECUTIVE SUMMARY

Dresden Nuclear Station Units 1. 2 and 3

iiRC Inspection Report 50-10/96014: 50-237/96014: 50-249/96014

This routine resident inspection included aspects of licensee operations.

maintenance, engineering, and plant support. The report covered a 7-week

period of resident inspection.

Doerations

. The facility was operated in a safe manner and previously identified

minor deficiencies were corrected (Section 01.1).

. The Unit 3 low pressure heater bay had improved accessibility and

housekeeping; however, minor material deficiencies were identified by

the inspectors (Section 01.2).

. A manual reactor trip was initiated in response to a loss of the 3B

reactor recirculation motor generator set. Plant and safety equipment

functioned as expected (Section 02.1).

. Unit 3 emergency diesel generator (EDG) ejected a cylinder test valve

after a surveillance run. No personnel injuries or significant damage

resulted and after minor repairs the EDG was returned to service

(Section 02.2).

Maintenance

. In general, maintenance activities were well controlled: however, two

work stoppages were issued due to non-safety related parts control and

contractor work practices (Section M1.1).

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. Significant repair work on the 3B reactor recirculation pump motor was l

well executed and managed. Root cause for the motor failure was foreign  !

material intrusion into the stator windings (Section M2.1). l

. Construction era rag was found inside the Unit 3 high pressure coolant

injection (HPCI) lube oil cooler waterbox. Tube leaks were repaired and

the system was restored to service (Section M2.2).

Enoineerina

. The licensee failed to perform post-modification testing on the Unit 2/3

main control room heating, ventilation and air conditioning (HVAC)

system. This was an apparent violation (Section E2.1). l

. An engineer failed to enter vendor technical information into the vendor

equipment technical information program (VETIP) as required by plant l

procedures (Section E4.1).

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Ins)ector review of two tem)orary alterations identified some problems

wit 1 implementation and tecinical evaluation (Section E4.2).

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Plant Support

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Computer accounting system failed at the beginning of the plant assembly

drill causing confusion. A thorough drill critique identified

deficiencies and corrective actions (Section P4.1).

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Problems were identified with the level indication and switch

calibration on the Unit 1 diesel-driven fire pump (Section F2.1). '

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REPORT DETAILS

Summary of Plant Status

Unit 2 began the period at a reduced load of about 300 MWe as some

maintenance activities were concluded. The unit was returned to full

power on October 22. On October 27 a 2% power derate was initiated due

to feedwater flow instrument uncertainty. On November 23 a load drop

was made to facilitate a drywell entry to add oil to the 2A reactor

recirculation pump motor. The unit was returned to near full power the

following day. On November 26 the 2% derate was lifted and the unit

returned to full power. On November 28. power was reducea for changing

condensate demineralizes and exercising control rod drives. The unit  :

began a slow power increase on December 2 and returned to full power on

December 3.

Unit 3 commenced this inspection period in coastdown in preparation for

refueling outage D3R14. On October 26. the 3B motor generator (MG) set

tripped and after a short period of single loop operations the reactor

was manually tripped on October 27. and a forced outage commenced.

I. OPERATIONS

01 Conduct of Operations

01.1 General Comments (71707)

Routine day-to-day facility operations were observed by inspectors both

in the control room and in the field. Main control board walkdowns and

reviews of various operating logs were also performed. Previous l

observations discussed in Inspection Re) ort 50-237/249-96013. dated

December 31. 1996 regarding minor breacdowns in control room decorum. l

3-way communications, and responsiveness to annunciators were not

observed during this inspection period. Generally, operator performance

inside the control room continued to be crisp and professional. A

weakness was noted with operations personnel outside the control room. 1

specifically, operator knowledge of the Unit 1 diesel-driven fire pump  ;

day tank level switches (paragraph F2.1).

01.2 Tour of Low Pressure Heater Bay (Unit 3)

a. Insoection Scone (71707)

The inspectors toured Unit 3 low 3ressure heater bay and observed the

general material condition houseceeping, and temporary alterations

installed on heater drain valves.

b. Observations and Findinos

Overall the inspectors noted significantly improved housekeeping over

the past nine months; however, numerous undocumented material

discrepancies were identified. These discrepancies included valves

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missing packing gland fasteners. open junction and electrical cable pull

boxes. and misadjusted piping hangers. After a discussion about general

conditions, several items were identified to the licensee for

correction.

Followup tours of the Unit 3 LP heater bay found that the specific items

had been addressed and a few additional items had been identified by the

licensee. One of the additional items identified by the licensee was an

o)en lighting junction box above one of the room exits. The tag for

t11s item was attached to a cable tray protective cover through a hole

where the cover bolt and stud had broken off. Additionally. the cover

had several loose or broken nuts, however, none of these deficiencies l

were identified by the licensee. l

c. Conclusions

The significant improvement in the housekeeping of the LP heater bay

allowed a greater portion of the room to be more easily accessible. The

reduction in contaminated areas further improved accessibility to the

room. However, the identification of material condition problems in

less traveled areas of the plant continued to be a challenge.

02 Operational Status of Facilities and Equipment

02.1 Recirculation Motor-Generator (MG) Set "B" Trio (Unit 3)

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a. Insoection Stone (71707)

On October 26. at 1758 the 3B Recirculation pump tripped due to tri) ping

of the 3B MG set. Onsite response to this event was performed by t1e

inspectors, and observation of control room personnel performance during

the power reduction and manual reactor scram was accomplished. The

following operational procedures were reviewed:

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Dresden Annunciator Procedure (DAN) 903-4 A6. 3B RECIRC M-G SET

GEN LOCKOUT.

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DAN 903-4 A7. 3B RECIRC PP DP LO.

. DAN 903-4 08, 3B RECIRC PP LOWER LUBE OIL LVL LO.

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Dresden Operating Abnormal (DOA) 0202-01. Recirculation Pump Trip

One or Both Pumps.

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Dresden General Procedure (DGP) 02-01. Unit 2 (3) NORMAL UNIT

SHUTDOWN

. DGP 02-03. REACTOR SCRAM

. DGP 03-03. SINGLE RECIRCULATION LOOP OPERATION

b. Observations and Findinos

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l The root cause of the MG set trip was not immediately known and single 1

l loop operation commenced. The inspectors responded to the site and i

monitored the reactor down power and the subsequent manual reactor trip I

at 0201 on October 27. After the 3B MG set tripped, the 3A MG set was

reduced to 60 percent power in accordance with approved procedures and

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the unit was stabilized at about 34 percent power. Power was further

decreased to 25 percent using recirculation flow and a manual reactor trip signal initiated. Systems responded as expected with the exception

of rod position indication failures for two rods and two intermediate

range monitor failures. For the evolutions observed plant operators

followed all appropriate procedures during the course of the shutdown.

Control room decorum and 3-way communications were maintained throughout

the event.

c. Conclusion

The plant response to the loss of a single reactor recirculation pump

was in accordance with expectations and plant design. The control room

operators followed procedures and conducted an orderly shutdown.

02.2 Emergency Diesel Generator (EDG) E.iected a Cylinder Test Valve Durina

Troubleshootina Run (Unit 3)

a. Inspection Scone (71707)

The inspectors observed a test of the Unit 3 EDG and observed the

licensee's response to the observed test failure. Field observations,

system and equipment inspection walkdowns were performed before and

after the valve ejection occurred. Additionally, the inspectors

reviewed the following documentation

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. Vendor Equipment Technical Information Program (VETIP) Manual

1163. Electro-Motive Diesel Engine.

.

Dresden Electrical Surveillance (DTS) 6600-01. Diesel Generator

Governor Oil Change and Compensation Adjustment

. Dresden Operations Surveillance (DOS) 6600-01. " Diesel Generator

Surveillance Test."

b. Observations and Findinas

On November 24. the inspectors observed performance of Dresden

Electrical Surveillance (DTS) 6600-01 for the Unit 3 EDG. No

abnormalities were noted during the initial performance of the test.

Subsequent to test performance, the Shift Manager informed the

inspectors that the EDG had ejected a cylinder test valve from

Cylinder 20. The High Voltage Operator (HVO) had entered the room to

secure the EDG and reported that the test valve had blown out. The

inspectors returned to the Unit 3 EDG room shortly after the EDG was

secured.

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The test valve had blown out of Cylinder 20 on the EDG generator end.

The valve appeared to have impacted the wall directly adjacent to the

valve and fallen to the floor. No damage was evident from the valve

ejection, other than carbon buildup on piping near the cylinder test

valve port. Inspection of the test valve showed no damage or unusual

wear. No personnel injuries were reported and the licensee immediately i

initiated a prompt investigation into the event. )

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l During additional inspection on November 25. the inspectors noted that

the Unit 3 EDG cylinder test valves did not appear to be threaded into i

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l the cylinder block as far as the test valves on the Unit 2 or 2/3 EDGs. 1

This information was conveyed to the licensee's team performing the  !

prompt event investigation.

l The prompt investigation c termined that the test valves had been j

replaced in December 1995, and that the ejected valve must have had a ,

relaxed torque that was further loosened due to normal EDG vibrations. '

Additionally. Cylinder 20 on the Unit 3 EDG was the cylinder with the

highest compression pressure on the engine. The licensee did not

perform a formal root cause evaluation of this event although several

corrective actions were performed. The EDG was repaired and was i

returned to service on November 27.

c. Conclusions

Operations personnel performed the surveillance testing in accordance

with the appropriate procedures and were observed closely monitoring EDG

performance.

08 Miscellaneous Operations Issues (92700)

08.1 (Closed) Violation (50-237:249/95010-03): Control of Overtime Not

Implemented In Accordance With Generic Letter (GL) 82-12. Revision 1 to

Dresden Operating Procedure 01-09. Control of Overtime authorized

November 14, 1995, incorporated the guidance established in GL 82-12.

This action appeared adequate to prevent recurrence: however, the

recently completed independent safety inspection (ref. IR 50-237:249/96-

201, dated December 24, 1996. Section 6.3.3) identified continuing

problems with corrective action for control of overtime. This item is

closed and further followup will be documented against Independent

Safety Inspection (ISI) Deficiency 50-237:249/96-201-29

08.2 (Closed) Insoector Followuo item (IFI) 50-237:249/96002-04: Atmospheric

Containment Atmosphere Dilution (ACAD) Operating and Surveillance

Procedures' Bands Differ. The inspectors noted that the ACAD system air

receiver operating pressure band was being maintained at 44 to 57 psig,

which was above the band in Dresden Operating Procedure (DOP) 2500-01.

"ACAD Dilution Subsystem Operation" (41 to 52 psig). Dresden Operating

Surveillance (DOS) 2500-01. "ACAD Compressor Surveillance," and Dresden

Administrative Technical Requirements (DATR) both listed a pressure band

of 44 to 57 psig. To resolve this issue, the licensee planned to revise

the appropriate ACAD procedures. The inspector reviewed the revised

ACAD procedure (DOP 2500-01) and the changes to the UFSAR and had no

further concerns. This item is closed.

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II. Maintenance

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M1 Conduct of Haintenance l

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M1.1 General Comments (62707)

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In general, maintenance activities at the facility were well controlled 1

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and performed in accordance with approved work packages and procedures. 1

Numerous tasks were observed in the field and minor observations were i

discussed with the appropriate licensee staff. Scheduling and work

planning continued to be difficult 3roblems. This was evident when a

stop work order was issued during t1e conduct of maintenance which left

an oil pump for both the 2A and 2B MG set oil skids out of service,

thereby leaving both MG sets in a more vulnerable condition. i

Significant work activities that were performed during this inspection .

period not receiving specific comment included the following; l

. 3D Electromatic Relief Valve Flange Leak Repair

. Unit 3 EDG Power Pack Replacement

Additionally, during this report period the licensee issued two stop

work orders. The first, issued November 21. regarded the retraining of l

contractor personnel in the use of nuclear standard work procedures. i

This was in response to a failure of contract worker personnel to comply l

with facility safe work practices. The second, issued November 24

regarded the procurement and use of non-safety related parts. This was

partially in response to the 3A control rod drive pump discharge

isolation valve that was installed with a through wall pinhole leak.

Both work stoppages were of short duration and were appropriate

resomses to address specific maintenance problems.

H2 Maintenance Material Condition of Facility and Equipment

M2.1 "B" Reactor Recirculation (RR) Pumo Motor Repair (Unit 3)

a. Inspection Scope (62707)

During the report period, the inspectors observed licensee actions to

troubleshoot and repair the 3B reactor recirculation (RR) motor trip.

Portions of the field preparation and actual repair were observed by the

inspectors. In addition, work package preparation and s3ecial rigging

and load testing documentation were reviewed including t1e following:

. Vendor Manual GEK-26132. " Boiling Water Nuclear Reactor

Recirculating Water Pump Motors for the Dresden 11 and III nuclear

power station of the Commonwealth Edison Company by the General

Electric Atomic Power Equipment Department."

. Special Procedure (SP) 96-11-019. "3B RR Pump Motor In-place

Repair."

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Motor Refurbishment - Details for the Engineered Impact Mat -

Unit 3."

. Dresden Engineering Document 5257492. " Reactor Recirculation Pump

Motor Refurbishment - Details for Pump Bowl Shimming. Engineered

Impact Mat and Rigging."

. Dresden Engineering Document 5253222. " Rigging of the 3B Recir.

Pump Motor End Bell. Rotor and Stator to Repair the Motor in

Place."

b. Observations and Findinas

After the October 26, 3B RR pump MG set trip. the licensee's ,

troubleshooting effort located a ground in the pump motor. Two l

approaches to resolve the problem were developed; repair the motor in- '

place, or replacement with a rebuilt motor. A rebuilt motor was

obtained and brought to the site, but work to repair in-place continued.

The repair work included load-testing the drywell monorail: design. l

testing, and installation of an engineered impact mat: development of a  !

rigging plan for the motor endbell, rotor and stator; and identifying j

possible repair techniques. The plan called for the removal of the  !

motor endbell and rotor and the lifting of the stator. The stator

needed to be lifted high enough to allow access for inspection and  !

repair. Once the package was finally prepared, a special )lant  !

operations review committee (PORC) reviewed and approved t1e plan.  !

During the preparation of the work, the inspectors reviewed selected

portions of the packages and observed monorail and impact mat testing. j

The use of a computer-generated animation of the lifting process greatly 1

aided all personnel in understanding the job. Also, the assignment of

the Operations Manager as a dedicated project manager ensured continuity

on the project.

During the stator inspection a small piece of banding material was

discovered shorting one motor phase. The foreign material was removed

and the damaged area of the windings repaired. After successfully

testing the windings, the motor was reassembled. The piece of banding ,

material most likely entered the motor in late 1990 to early 1991 time l

frame when the endbell had been removed for maintenance. The banding

material was similar to material used to secure component identification

label plates inside the drywell. The licensee suspected that some of

this material was dropped into the motor and eventually shorted the

stator. Additional foreign material found inside the motor was removed.

The intrusion of foreign material into various components at the

facility has been a longstanding problem. However, the inspectors'

recent observations of foreign material exclusion (ME) practices

indicated that significant improvements have been made over past

practices.

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The ins)ectors observed various activities as the work progressed and

noted tlat the job was well managed and skillfully performed.

Disassembly, re) air. and reassembly progressed as expected and no major

problems with t1e work plans were encountered. Radiation protection

controls and practices were followed and the use of a video monitor for

t the viewing of the work was a good "as low as reasonably achievable"

l (ALARA) practice.

c. Conclusions

The 3B RR pump motor repair was well coordinated. Management and Site

Quality Verification oversight were maintained and no significant

! unanticipated problems occurred. The finding of several pieces of

foreign material inside a major component was not a new issue at the

facility and efforts to improve FME continued to receive appropriate

management attention.

M2.2 Rao Found in Hiah Pressure Coolant Iniection (HPCI) Lube Oil Cooler.

(Unit 2)

a. Inspection Scone (62707)

The inspectors ins)ected the Unit 2 HPCI lube oil cooler and observed

the rag found by t1e licensee during emergent maintenance work. A

review of the licensee's efforts to identify when the rag entered the

system was also performed,

b. Observations and Findinas  !

The HPCI system was declared inoperable on November 27. due to excessive l

water contamination in the turbine lubricating oil. While performing i

maintenance to repair the water leaks in the lube oil cooler,

maintenance personnel discovered a rag in the cooler water box. The rag

covered a significant portion of the cooler tube openings and appeared

to have been acting as a filter for the cooling medium.

The licensee suspects that the rag had been used as an FME cover during

facility construction and was never removed. The assumption was

substantiated due to the lack of finding any previous maintenance items

that required removal of the HPCI lube oil cooler endbells in the

maintenance database. Further database searches showed that no recorded

maintenance work had been performed on the cooler or cooling system that

would have allowed visual identification of the rag since the system was

originally placed in service. The licensee also reviewed surveillance

test data and did not identify any instance of the HPCI system being

inoperable or degraded due to inadequate lube oil cooler performance.

Repair efforts were completed and the cooler was reassembled and

satisfactorily tested. Unit 2 HPCI was returned to service on

December 1, with no further problems.

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c. Conclusions

i- All observed maintenance activities were performed in a skilled manner,

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however, the discovery of the rag in the cooler further emphasized the

i need to continue monitoring FME controls.

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M8 Miscellaneous Maintenance Issues (92902) I

i M8.1 (Closed) Insoector Followuo Item 50-237/249-95008-01: Failure to Follow

Procedure Resulted in Two Inoperable Core Spray Systems. On April 24, '

1995, the licensee reused o-rings on environmentally qualified equipment l

} and only hand tightened the transmitter covers in violation of the l

3rocedure. The inspectors reviewed information on reused o-rings and )

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land tightened covers in CHRON # 0308805 and a referenced letter from '

i Rosemount. The information a)peared adequate to support the licensee's

l operability determination. T11s item is closed.

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III. Enaineerina

E2 Engineering Support of Facilities and Equipment

E2.1 Failure to Perform Adeouate Post-Modification Testina of the Control

Room Heatina and Air Conditionina (HVAC) System (Units 1. 2 and 3)

a. Insoection Scope (37551)

The inspectors continued to observe and monitor the licensee's progress

in correcting control room HVAC design and testing deficiencies. The

following documentation was reviewed:

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Modifications M12-2/3-82-1. M12-0-87-005 and M12-0-86-006: Unit 1

Control Room Modifications.

  • DTS 5750-06, " Control Room Standby HVAC Air Filtration Unit, and

Refrigeration Condensing Unit Performance Requirements," dated

August 24, 1996.

b. Observations and Findinas

The licensee continued work on sealing penetrations into the Unit 2/3

control room, auxiliary computer room, and train "B" HVAC rcom. At the

close of this report period, efforts to remove a temporary alteration

and return the auxiliary computer roo.n into the control room envelope

were unsuccessful. The licensee continued testing and achieved and

maintained positive pressure requirements with the exception of the

auxiliary computer room. Further work was planned to correct problems

in the computer room and return the room to the control room envelope.

Background information on this issue can be found in Inspection Report

96013 (paragraph E2.4) and Independent Safety Inspection (ISI) Report

96-201 (paragraph 4.6.4.1). The significance of this event was

previously considered an Unresolved Item (50-237:249/95013-02).

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c. ISI Report 96-201. dated December 24. 1997. Daragraoh 4.6.4.1

Sections 6.4.2 and 9.4-3 of the UFSAR described the design basis for the

control room HVAC system. Section 6.4.2.4 stated that potential adverse

interactions between the control room emergency zone and adjacent zones

that may allow the transfer of toxic or radioactive gases into the

control room were minimized by maintaining the control room at a ,

positive pressure of 1/8-inch water gauge (iwg) during emergency l

pressurization modes, and with respect to adjacent areas.

On October 8. 1996, the licensee declared the control room HVAC system

inoperable because of the inability to maintain the control room at a

positive pressure during normal operations and at 1/8 iwg with respect

to the surrounding areas in the emergency mode. The control room

ventilation system had not been maintained or properly tested 'o ensure

that the system operated within its design basis. Modifications had

been implemented, or partially implemented, which resulted in negative

pressure within the control room and the inability to pressurize the l

control room to 1/8 iwg in the emergency mode. In addition,

instrumentation that was used to verify the control room pressure was

positive in the emergency mode had not been calibrated, and had not been

installed in accordance with the piping and instrumentation diagram. j

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In September 1996, the licensee began reviewirg open modifications for '

the control room ventilation system, and subsequently determined that

several control room modifications, which had not been completed, i

contributed to the inability to pressurize the control room as stated in

the UFSAR. These incomplete modifications were identified as a result ,

of the licensee's efforts to close all modifications or approve the as- I

built configuration. The specific modifications affecting the control

room included:

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M12-0-87-005-D provided for the installation of security equipment

such as bullet resistant plating for walls and ceilings, new east- l

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west kitchen and locker room area fire and non-fire rated doors. I

and the sealing of new and unused wall and floor penetrations.

Field work was initiated in August 1991 and completed in j

January 1992. Post-modification testina was not oerformed.

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. M12-0-87-005-E provided supply and exhaust ventilation systems for i

the new locker room and kitchen areas, new fire dampers in duct

work penetrating fire walls, control logic for operation of the

isolation dampers, and an interlock for the exhaust fans from the

isolation dampers. Field work was started in September 1991 and l

completed by June 1993. The oost-modification testina, includina

loaic testina and emergency oressurization testina to verify

1/8 iwa was not oerformed.

. M12-0-86-006-C provided supply and return side duct silencers, j

thermally insulated duct work, and manual volume dampers in the

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shared return duct works. The field work was started in  !

March 1989 and the documentation closure was completed in  !

September 1993. Post-modification testina was not comoleted.

. M12-0-86-006-D provided for the removal of existing HVAC duct work

supports inside the Unit 2 and 3 control room, installed I

acoustical tile, installed new duct work including hangers and

safety chains. reworked existing ductwork inside the control room,

and removed existing butterfly dampers inside the control room.

The field work was initiated in June 1989 and the work was l

determined to be completed in May 1993. Post-modification testina

was not completed

. M12-2/3-82-1 added the HVAC Train B in 1982; however, the NRC's

ISI team concluded the modification was not adeouately tested. l

Surveillance Procedure (DTS) 5750-06. Revision 3. " Control Room Standby

HVAC Air Filtration Unit, and Refrigeration Condensing Unit Performance

Requirements." dated August 24, 1996, only required 1/8 iwg positive

pressure in the control room and did not ensure thst pressure was .

greater than 1/8 iwg for the surrounding areas. In addition, the l

instrumentation used to verify the control room differential

pressure (d)) was not calibrated nor verified to be appro)riate for the

parameters Jeing measured. Specifically, dp Instruments )PI-2-5740-

31/32 and 36 for the control room and east turbine building had not been

calibrated. The licensee also identified that the control room

instrumentation was mislabeled with respect to the areas being sensed

and, according to '.he drawings, other sensing lines were misrouted or

were broken.

d. Conclusions

The licensee's failure to perform testing of modifications performed to

Unit 2/3 control room HVAC system, as discussed above and detailed in

the ISI Irspection Report 96-201, section 4.6.4.1. dated December 24.

1996, is an Apparent Violation of 10 CFR 50. Appendix B. Criterion XI.

" Test Controls." (50-237/249-96014-01).

The apparent violation is being considered for escalated enforcement

action in accordance with the " General Statement of Policy and Procedure

for NRC Enforcement Actions" (Enforcement Policy). NUREG-1600.

Accordingly, no Notice of Violation is presently being issued for this

inspection finding. The significance of the issue, and short term

corrective actions were discussed with the licensee in the exit meeting

for this inspection period on December 19. 1996.

Before the NRC makes an enforcement decision, the licensee will be

provided an opportucity to respond to the ap)arent violation at a pre-

decisional enforcement conference as descri)ed in the cover letter to

this report.

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E3 Engineering Procedures and Documentation

E3.1 Additional Vodated Final Safety Analysis Report (UFSAR) Discreoancies

a. Insoection Scooe (71707)  :

The inspectors used the UFSAR as a technical reference during a review

of findings' from a routine drywell tour. A comparison of actual plant

configuration was made to the descriptions contained in the UFSAR. Note

that other UFSAR discrepancies regarding the control room HVAC system

were documented in Section E2.1.

l b. Observations and Findinos j

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! Prior to performing a Unit 3 drywell routine tour the inspectors

l reviewed various UFSAR sections including section 6.1.1.1 " Materials

Selection and Fabrication." This section stated, "All piping inside

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containment is covered with metallic mirror-type insulation." During

the drywell tour the inspectors found this not to be the case as several

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other types of insulation were used on piping. The licensee confirmed

that the other types of insulation ident1fied by the inspectors were

acceptable for use in the drywell. This discrepancy was discussed with

the licensee and a change to the UFSAR and a performance improvement

form (PIF) were initiated.

c. Conclusion

The above example showed that discrepancies between plant configuration

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and the UFSAR still exist. However, the licensee was taking prompt

actions to resolve identified discrepancies.

E4 Engineering Staff Knowledge and Performance

E4.1 Failure to Uodate Emeraency Diesel Generator (EDG) Vendor Technical

Information Manual (Units 2 and 3)

a. Insoection Scooe (37551)

While inspecting the licensee's response to a Unit 3 EDG test valve

failure (Section 02.2 of this report), the inspectors reviewed the l

approved vendor technical manual. The inspectors compared the approved

vendor manual to the conditions that existed in the field and conducted-

discussions with the system engineer and engineering management. The

following administrative procedures were also reviewed;

e Dresden Administrative Procedure (DAP) 02-10. " Control of Vendor

Equipment Technical Information," Revision 5.

. Nuclear Engineering Procedure (NEP) 07-04. "VETIP Process

, Control," Revision 0.

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b. Observations and Findings l

The inspectors noted that the test valves depicted in the manual were

different from those installed on the EDGs. During discussion with the  :

licensee, the correct information was found in the system engineer's

desk. Maintaining vendor supplied technical information in an

uncontrolled manner was contrary to the licensee's vendor equipment l

technical information program (VETIP). Dresden Administrative  !

Procedure 02-10. Revision 5. Section E.5 required that " Existing, i

uncontrolled, and ircoming ETI (Equipment Technical Information) shall

be reviewed and added to VETIP so that the latest /most applicable )

information is available for station use." l

In addition. NEP 07-04. Section 5.2.1.2. required that "The person

receiving new vendor manual revision data shall forward the information

to the VETIP Coordinator attached to the VETIP Authorization Form

(Exhibit A) or suitable equivalent."

The licensee initiated a PIF documenting the misplaced vendor data and  ;

forwarded the information to the VETIP coordinator for inclusion into  !

the EDG VETIP manual. ,

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c. Conclusions l

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Past weaknesses in the VETIP program were previously documented in

Inspection Report 96006. section M2.1. dated August 22 1996. The l

licensee was not successful in assuring the VETIP was hroperly i

implemented. Not entering the EDG test valve technical information l

change into the VETIP program as required by approved procedures was a

Violation of Technical Specification 6.2. Procedures and Programs

(50-237/249-96014-02). 1

E4.2 Review of Temocrary Alterations Related to the Control Room HVAC Repair I

and the 125Vdc and 250Vdc Batteries (Units 2 and 3)

a. Insoection Scooe (37551)

The inspectors reviewed two installed temporary alterations. The review

included a field walkdown of the alterations and a review of the

associated documentation and procedures including:

. DAP 05-08. " Control of Temporary System Alterations."

. Temporary Alteration No. III-53-96. " Isolate HVAC Supply / Return To

and From the Aux Computer Room."

. Temporary Alteration No. III-33-96. " Supply Temporary Heat to U2

125V and 250V DC Battery Rooms."

b. Observations and Findinos

The auxiliary computer room temporary alteration was installed to

isolate the room from the control room while the control room walls were

i sealed. The temporary alteration called for three portable air

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conditioning (AC) units to be placed in the room and vented out the

auxiliary computer room door. During the walkdown, the inspectors noted

that the door to the room was left open to accommodate the three exhaust

trunks used to expel heated exhausts from the portable AC units. This

arrangement essentially countered any benefit received from the AC units

because of the free exchange of warmer auxiliary electrical room air

into the auxiliary computer room. l

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The Unit 2 battery rooms temporary alteration was installed to ensure

that the proper temperature was maintained in the battery rooms while

work was in progress on the normal ventilation system. During the

walkdown, the ins)ectors observed that the alteration had been installed

as intended and tlat a firewatch was present. Both doors to both

battery rooms were also open which, although allowed by the temporary

alteration. seemed unnecessary and even counterproductive to the

intended design.

Additionally, the inspectors noted that the battery rooms were about

81 F. well abon the required tem)erature of 68 F. This observation was

conveyed to the licensee and the )attery rooms were returned to normal

and the firewatch secured. Subsequently, room temperature was monitored

by hourly operator rounds.

A documentation review showed that the technical evaluation had been

identified as not safety related. The documented explanation stated

that the batteries were safety-related, but the room HVAC system was

not.

The 125V and 250V batteries were the most risk significant system at the

facility and were clearly safety-related. The temporary alteration was

only concerned with maintaining the room temperatures above 68 F to

assure the batteries were not in a degraded condition. Therefore. the

installation of the temporary alteration directly affected the two

station batteries not just the room HVAC. I

c. Conclusions

Although the alterations were installed as written, the design

effectiveness was flawed. This appeared to be the result of an

ineffective field walkdown of the alteration and a weak review of the

design implementation. Additionally, the licensee maintained that the

battery room alteration only affected the battery room HVAC system and '

was not safety-related. Further discussions will be needed to resolve

this issue: therefore this issue will remain an Unresolved Item

(50-237/249-96014-03).

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E6 Engineering Organization and Administration l

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E6.1 Enaineerina Deoartment Manaaement Chances (37551)

, A new Site Engineering Manager, Mr. Russell Freeman, was ao)ointed 1

l during the report period. Previously. Mr. Freeman was the )resden Plant  ;

l Engineering Superintendent.

E8 Miscellaneous Engineering Issues (92903)

E8.1 (Closed) Unresolved Item (50-237/249-95015-05): Corner Room Steel.  !

This issue regarded the corrective action for inadequate corner room l

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structural steel design margins, and was the subject of escalated  ;

enforcement and a civil penalty (EA 96-115) on June 13, 1996. This item  !

is closed.  !

E8.2 (Closed) Unresolved Item (50-237/249-96013-02): Control Room i

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Ventilation System Operability. This issue regarded the licensee's I

corrective actions to resolve inadequate post-modification testing of

the control room HVAC system. This issue was reviewed and is an example

of an apparent violation discussed in Section E2.1 of this re) ort.

Additional followup of this item will be documented against tais reports  !

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assigned tracking number. This item is closed.  !

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IV. Plant Suooort

P4 Staff Knowledge and Performance in EP '

P4.1 Performance durina Assembly Drill (Units 1. 2 and 3)

a. Inspection Scoce (82701)  ;

On November 26 the inspectors observed licensee response to an ,

unannounced site assembly drill. Documents reviewed included Emergency

Plant Im)lementing Procedures (EPIP) 0400-01, " Plant Assembly and i

Accounta)ility."

b. Observations and Findings

The station alarm was sounded at 1230 and the site assembly drill was

announced on the station public address system. The inspectors

responded to assigned assembly points and noted that the computerized

assembly card reading system was not operating. After being manually

accounted, the inspectors went to other assE.3bly areas to observe

activities.

l In the Administrative Building the accounting 3rocess was in disarray.

The lunchroom and main hallway were filled wit 1 personnel waiting to be

counted. Twenty minutes into the drill the licensee initiated a manual

l accounting of personnel in the Administration Building. This was ,

accomplished by handing out sheets of paper to management personnel and

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requiring managers to count assigned personnel. At one point a station

supervisor directed assigned personnel to leave the Administration

Building and go to a work area. This was followed by similar direction

from another su)ervisor. The individual in charge of the accountability

activities in t1e Administration Building halted the exodus and stated

that the accounting for all groups would be completed in the

Administration Building.

The licensee was able to gain control of the accounting process;

however, the licensee was not able to complete the accounting within the

allotted time. Station management determined that aerformance during

the drill was unsuccessful and another drill was scleduled. The

licensee's critique was thorough and independently addressed all of the

inspectors' concerns.

c. Conclusions

The difficulty the licensee experienced in accounting for the station

staff manually demonstrated the there had been an over-reliance on the

computer counting. The licensee's thorough post-drill critique

correctiy assessed the weakness in performance and established

appropriate corrective actions.

F2 Status of Fire Protection Facilities and Equipment

F2.1 Problems Identified with Diesel-Driven Fire Pumo (Units 1. 2 and 3)

a. Insoection Scope (64704)

The inspectors performed walkdowns of the Unit 1 diesel-driven fire pump

and all associated equipment and held several discussions with licensee

staff. The following documentation was also reviewed:

. DAN 901-2 E-8. "U1 Fire PP Day Tank Lvl Hi."

.

Dresden Fire Protection Surveillance (DFPS) 4123-01. " Unit 1

Diesel Fire Pump Operability."

. Schematic Diagram 12E-6580F, " Fire Protection System Diesel Driven

Fire Pump Intake Structure."

. Wiring Diagram 12E-6580G. " Diesel Driven Fire Pump."

b. Observations and Findinos

On November 15. the Unit 1 diesel-driven fire pump failed a surveillance

run. The cause for the failure was the closing of the fuel su) ply

solenoid valve that occurred when a power lead to the valve vi] rated off

a terminal. During subsequent walkdowns of the pump and associated

components. the inspectors questioned if the local fuel oil storage tank

level float was operating 3roperly. The work execution center (WEC)

supervisor was contacted a)out the level indicator and stated that the

indicator was working properly. Upon further investigation, the

licensee determined that the level float was not operating properly.

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The installed level float indicated the tank was between 3/4 and 7/8

full, when the tank was only a little more than half full.

The inspectors also questioned the low level alarm switch calibrations

and requested the latest calibration records. The same WEC supervisor

was contacted and stated that there was a high level alarm but no low

level alarm on the tank. The inspectors reverified that there was a low

level switch, a high and a high-high level switch. The licensee then

determined that the level switches were not in the calibration 3rogram

and could not find any documentation of the switches being cali) rated.

The fuel tank local level indicator float was repaired and the level

switches were calibrated. The solenoid power lead was reterminated and

the Unit 1 diesel-driven fire pump successfully passed surveillance

testing and was returned to service. '

c. Conclusion

The fire protection system has had numerous problems over the last few

months and did not appear to be receiving an adequate level of

attention. The system operation was not fully understood by some

members of the plant staff.

F8 Hiscellaneous Fire Protection Issues (92904)

F8.1 (Closed) IFT 50-237/249-95008-10: Emergency Lighting. During a fire

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protection inspection, the ins)ectors identified that several emergency

lights were dirty, several lig1ts were aimed improperly, and one light

was blocked by a plant modification. The licensee permanently relocated

the blocked emergency light to a new location. The affected emergency

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lights were correctly aimed. Also, a procedure change was completed to

Dresden Electrical Surveillance (DES) 4153-02. Safe Shutdown Emergency

Lighting Quarterly Inspection, to ensure that emergency lights' lamps

would be inspected and cleaned as necessary. This item is closed.

VI. Manacement Meetinas

X1 Exit Meeting Summary

"

The inspectors 3 resented the inspection results to members of licensee

management at t1e conclusion of the inspection on December 19. 1996.

The licensee acknowledged the findings presented.

The inspectors asked the licensee whether any materials examined during

the inspection should be considered proprietary. No proprietary

information was identified.

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PARTIAL LIST OF PERSONS CONTACTED !

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l Licensee

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' S. Perry. Vice President. BWR Operations  !

l E. Connell. Design Engineering Superintendent  ;

! T. Foster. Work Control and Outage Manager 1

R. Freeman. Plant Engineering Superintendent  !

l J. Heffley. Units 2 and 3 Station Manager ,

C. Howland. Radiation Protection Manager l

R. Kundalkar. Site Engineering Manager

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T. Nauman. Unit 1 Station Manager l

T. O'Connor. Operations Manager i

F. Spangenburg Regulatory Assurance Manager I

P. Swafford. Unit 2/3 Maintenance Superintendent

P. Tzomes. Support Services Director  :

D. Winchester. Safety Ouality Verification Director i

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INSPECTION PROCEDURES USED

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IP 37551: On-site Engineering i

IP 62707: Maintenance Observations

IP 64704: Fire Protection Program

IP 71707: Plant Operations

IP 82701: Operational Status of the Emergency Preparedness Program

IP 92901: Followup - Plant Operations

IP 92902: Followup - Maintenance

i IP 92903: Followup - Engineering

l IP 92904: Followup - Plant Support

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ITEMS OPENED AND CLOSED

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l 50-237/249-96014-01 APPARENT Failure to Perform Post-Modification Testing for

l VIO Control Room HVAC System (Apparent Violation).

l 50-237/249-96014-02 VIO Failure to Follow VETIP Procedure for Incoming l

Vendor Technical Information. 1

50-237/249-96014-03 URI Battery Room Temporary Alteration.

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Closed

50-237:249/95010-03 VIO Control of Overtime Not Implemented In

Accordance With Generic Letter (GL) 82-12.

50-237/249-95015-05 URI Corner Room Steel.

50-237/249-96013-02 URI Control Room Ventilation System Operability.

50-237/249-95008-01 IFI Failure to Follow Procedure Resulted in Two

Inoperable Core Spray Systems.  !

50-237/249-95008-10 IFI Emergency Lighting.

50-237:249/96002-04 IFI Atmospheric Containment Atmosphere Dilution

(ACAD) Operating and Surveillance Procedures'

Bands Differ.

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LIST OF ACRONYM 3 USED

AC Air Conditioning

i ACAD Atmospheric Containment Atmosphere Dilution

ALARA As Low As Reasonably Achievable I

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CFR Code of Federal Regulations  !

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CRD Coritrol Rod Drive I

! DAN Dresden Annunciator Procedure

1

DAP Dresden Administrative Procedure

4 DATR Dresden Administrative Technical Requirements

DES Dresden Electrical Surveillance

DFPS Dresden Fire Protection Surveillance

DGP Dresden General Procedure 1

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DOA Dresden Operating Abnormal l

DOP Dresden Operating Procedure

DOS Dresden Operations Surveillance

dP Differential Procedure

DTS Dresden Technical Surveillance

a EA Enforcement Action

EDG Emergency Diesel Generator

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EPIP Emergency Plan Implementing Procedures

ETI Equipment Technical Information

FME Foreign Material Exclusion
GL Generic Letter

HPCI High Pressure Coolant Injection

HVAC Heating. Ventilation, and Air Conditioning

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HVO High Voltage Operator

IFI Inspector Followup Item

ISI Independent Safety Inspection

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IWG Inches Water Gage

LP Low Pressure

MG Motor Generator

MMD Mechanical Maintenance Department

MWe Megawatts Electrical

NEP Nuclear Engineering Procedure l

J NDV Notice of Violation '

l PDR Public Document Room j

PIF Performance Improvement Form

PORC Plant Operations Review Committee

asig Pounds Per Square Inch Gauge

l 1R Reactor Recirculation

l UFSAR Updated Final Safety Analysis Report

i URI Unresolved Item

VETIP Vendor Equipment Technical Information Program

WEC Work Execution Center

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