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{{#Wiki_filter: | {{#Wiki_filter:O O | ||
VERMONT YANKEE NUCLEAR POWMR CORPORATION SEVENTY SCVEN OROVE STRECT RUTLAND, YEIO10NT 03701 REPLY TO: | |||
( | |||
VYV-3078 | VYV-3078 | ||
: p. o. Box 157 VERNON, VERMONT o5354 November 20, 1973 United States Atomic Energy Commission Directorate of Regulatory Operations, Region I 631 Park Avenue King of Prussia, Pennsylvania 19406 | : p. o. Box 157 VERNON, VERMONT o5354 November 20, 1973 United States Atomic Energy Commission Directorate of Regulatory Operations, Region I 631 Park Avenue King of Prussia, Pennsylvania 19406 | ||
==REFERENCE:== | ==REFERENCE:== | ||
Operating License DPR-28 Docket No. 50-271 Abnormal Occurrence No. A0-73-32 | Operating License DPR-28 Docket No. 50-271 Abnormal Occurrence No. A0-73-32 Gentlemen: | ||
Gentlemen: | |||
As defined by Technical Specifications for the Vermont Yankee Nuclear Power Station, Section 6.7.B.1, we are reporting the following Abnormal Occurrence as A0-73-32 and confirming our conversation with your inspecto,r. | As defined by Technical Specifications for the Vermont Yankee Nuclear Power Station, Section 6.7.B.1, we are reporting the following Abnormal Occurrence as A0-73-32 and confirming our conversation with your inspecto,r. | ||
On November 20, 1973, at 0620, during conduct of the monthly High Pressare. Coolant Injection (HPCI) System pump operability surveillance test, both gaskets on the gland seal exhaust condenser failed. This cooler is required for proper operation of the HPCI system and its loss precludes the HPCI operability required by Section 3.5.E.1.a of the Technical Specifications. The reactor was operating at approximately 62% power at the time of this incident. | On November 20, 1973, at 0620, during conduct of the monthly High Pressare. Coolant Injection (HPCI) System pump operability surveillance test, both gaskets on the gland seal exhaust condenser failed. | ||
This cooler is required for proper operation of the HPCI system and its loss precludes the HPCI operability required by Section 3.5.E.1.a of the Technical Specifications. The reactor was operating at approximately 62% power at the time of this incident. | |||
Replacement of the failed gaskets was initiated immediately. | Replacement of the failed gaskets was initiated immediately. | ||
Concurrently, the operability verification required by Section 4.5.E.2 | Concurrently, the operability verification required by Section 4.5.E.2 of Technical Specifications was begun. | ||
The cooler was repaired and HPCI was tested and verified operable at 0945. | The cooler was repaired and HPCI was tested and verified operable at 0945. | ||
Very truly yours, VERMONT YANKEE NUCLEAR POWER CORPORATION Q | Very truly yours, VERMONT YANKEE NUCLEAR POWER CORPORATION Q | ||
B.W. Riley Plant Superintendent WFC/kbd | B.W. Riley Plant Superintendent WFC/kbd d | ||
J 9312O20425}3 | L', | ||
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9312O20425}3 t | |||
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i 5" *" oowt t'"*- | i MEMO ROUTE SLIP 5" *" oowt t'"*- | ||
rorm Ai r-95 i n .. M., i 4. i v i ? > A t tu o2 4o | For coacu"*aa-F a' *"'oa-rorm Ai r-95 i n.. M., i 4. i v i ? > A t tu o2 4o Net...are,orn ror,ica.to,.. | ||
To (Name anJ uan) | S.' X rer vero,-,ioe. | ||
Central Mail & Files | To (Name anJ uan) imnia RtMARns VERMONT YANKEE NUCLEAR PORER CORPORATIOr RO Chief. FS6EB RO:HQ (5) 8"'E DN 50-271 RO Files s. | ||
To m.m..newno | Central Mail & Files Rannintorv senndards (3) | ||
A0 73-32 To m.m..newno | |||
.mnus REM. Ras The above abnormal occurrence is forwarded Directorate of Licensing (13) for information. Distribution will be made OGC DATE Regional Directors (Rn T T. TTT. TVT by this office to the PDR, Local PDR, NSIC, Td (Name ana unit) | |||
INTIALS REMARK $ | |||
DTIE, and' State Representatives. | DTIE, and' State Representatives. | ||
DATE FRO (Name ud unst) | DATE FRO (Name ud unst) | ||
[/. 0 && | REM ARKS | ||
W. J. Brunner Region I | [/. 0 && | ||
PHONE 84 | W. J. Brunner Region I PHONE 84 DATE 8-337-1246 12/4/73 USE OTHER SIDE FOR AD&4TIONAL REMARK $ | ||
CFO t 1,18 0 445-43 a e | |||
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Latest revision as of 02:26, 14 December 2024
| ML20086D623 | |
| Person / Time | |
|---|---|
| Site: | Vermont Yankee File:NorthStar Vermont Yankee icon.png |
| Issue date: | 11/20/1973 |
| From: | Riley B VERMONT YANKEE NUCLEAR POWER CORP. |
| To: | NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I) |
| Shared Package | |
| ML20086D625 | List: |
| References | |
| AO-73-32, VYV-3078, NUDOCS 8312020425 | |
| Download: ML20086D623 (2) | |
Text
O O
VERMONT YANKEE NUCLEAR POWMR CORPORATION SEVENTY SCVEN OROVE STRECT RUTLAND, YEIO10NT 03701 REPLY TO:
(
VYV-3078
- p. o. Box 157 VERNON, VERMONT o5354 November 20, 1973 United States Atomic Energy Commission Directorate of Regulatory Operations, Region I 631 Park Avenue King of Prussia, Pennsylvania 19406
REFERENCE:
Operating License DPR-28 Docket No. 50-271 Abnormal Occurrence No. A0-73-32 Gentlemen:
As defined by Technical Specifications for the Vermont Yankee Nuclear Power Station, Section 6.7.B.1, we are reporting the following Abnormal Occurrence as A0-73-32 and confirming our conversation with your inspecto,r.
On November 20, 1973, at 0620, during conduct of the monthly High Pressare. Coolant Injection (HPCI) System pump operability surveillance test, both gaskets on the gland seal exhaust condenser failed.
This cooler is required for proper operation of the HPCI system and its loss precludes the HPCI operability required by Section 3.5.E.1.a of the Technical Specifications. The reactor was operating at approximately 62% power at the time of this incident.
Replacement of the failed gaskets was initiated immediately.
Concurrently, the operability verification required by Section 4.5.E.2 of Technical Specifications was begun.
The cooler was repaired and HPCI was tested and verified operable at 0945.
Very truly yours, VERMONT YANKEE NUCLEAR POWER CORPORATION Q
B.W. Riley Plant Superintendent WFC/kbd d
L',
J 20
,t q
9312O20425}3 t
- ' (4 F S
t
)
i MEMO ROUTE SLIP 5" *" oowt t'"*-
For coacu"*aa-F a' *"'oa-rorm Ai r-95 i n.. M., i 4. i v i ? > A t tu o2 4o Net...are,orn ror,ica.to,..
S.' X rer vero,-,ioe.
To (Name anJ uan) imnia RtMARns VERMONT YANKEE NUCLEAR PORER CORPORATIOr RO Chief. FS6EB RO:HQ (5) 8"'E DN 50-271 RO Files s.
Central Mail & Files Rannintorv senndards (3)
A0 73-32 To m.m..newno
.mnus REM. Ras The above abnormal occurrence is forwarded Directorate of Licensing (13) for information. Distribution will be made OGC DATE Regional Directors (Rn T T. TTT. TVT by this office to the PDR, Local PDR, NSIC, Td (Name ana unit)
INTIALS REMARK $
DTIE, and' State Representatives.
DATE FRO (Name ud unst)
REM ARKS
[/. 0 &&
W. J. Brunner Region I PHONE 84 DATE 8-337-1246 12/4/73 USE OTHER SIDE FOR AD&4TIONAL REMARK $
CFO t 1,18 0 445-43 a e
I l
, w.e
-,