ML20062M715: Difference between revisions

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Pacific Gas and Electric Company 77 Bea!e Street                         Gregory M. Rueger San Francisco.CA 94106                 6enior Vice President and t
6-295lnep 46 323 OAL rze.
l 415/973-4684                    's r~r# q/c" General Manager Nuclear Power Generation l
r.- i Pacific Gas and Electric Company 77 Bea!e Street Gregory M. Rueger 6enior Vice President and San Francisco.CA 94106 r~r# q/c" General Manager
February 1, 1993                                      73 C M N ?
's 415/973-4684 t
PG&E Letter No. DCL-93-026 U.S. Nuclear Regulatory Commission ATTN: Document Control Desk Washington, D.C. 20555 Re:       Docket No. 50-275, OL-DPR-80 Docket No. 50-323, OL-DPR-82 Diablo Canyon Units 1 and 2 Licensee Event Report 2-87-023-01 (Voluntary)
Nuclear Power Generation l
l 73 C M N ?
February 1, 1993 PG&E Letter No. DCL-93-026 U.S. Nuclear Regulatory Commission ATTN:
Document Control Desk Washington, D.C.
20555 Re:
Docket No. 50-275, OL-DPR-80 Docket No. 50-323, OL-DPR-82 Diablo Canyon Units 1 and 2 Licensee Event Report 2-87-023-01 (Voluntary)
Accumulator Nozzle Cracking Due to Intergranular Stress Corrosion Gentlemen:
Accumulator Nozzle Cracking Due to Intergranular Stress Corrosion Gentlemen:
PG&E is submitting a revision to voluntary Licensee Event Report 2-87-023-00 concerning intergranular stress corrosion cracking in bah Units 1 and 2 accumulator nozzles. This revision is submitted to report the results of inspections and repair actions performed during the Unit 2 fourth refueling outage and the Unit 1 fifth refueling outage. This report is submitted for information purposes only as described in Item 19 of supplement I to NUREG-1022. Revision bars in the margin indicate the revised LER sections.
PG&E is submitting a revision to voluntary Licensee Event Report 2-87-023-00 concerning intergranular stress corrosion cracking in bah Units 1 and 2 accumulator nozzles.
This revision is submitted to report the results of inspections and repair actions performed during the Unit 2 fourth refueling outage and the Unit 1 fifth refueling outage.
This report is submitted for information purposes only as described in Item 19 of supplement I to NUREG-1022.
Revision bars in the margin indicate the revised LER sections.
This event has in no way affected the health and safety of the public.
This event has in no way affected the health and safety of the public.
Sincerely,
Sincerely,
                  'M       AW
'M AW
                                                                                                          -          .c Gregory M. Rueger cc:     Ann P. Hodgdon John B. Martin Mary H. Miller Sheri R. Peterson CPUC Diablo Distribution INP0                                           taucttAn Rtcui Aron cov:.tesion DC2-87-MM-N024                                            '@'Gd C"M En M -#M/'                   W DC2-91-TN-N075                        "*5d'N- /S 'D /hd $5M N M W D
.c Gregory M. Rueger cc:
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Ann P. Hodgdon John B. Martin Mary H. Miller Sheri R. Peterson CPUC Diablo Distribution INP0 taucttAn Rtcui Aron cov:.tesion
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1091S/85K/JCN/2246 cmmsh3YEj2dhm ?+'73
1091S/85K/JCN/2246 cmmsh3YEj2dhm ?+'73
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9401110149 930818                                                           '
9401110149 930818 PDR ADDCK 05000275 O
PDR ADDCK 05000275 O                   PDR
PDR


l'                                                       LICENSEE EVENT REPORT (LER)                                                       202672                       ,
l' LICENSEE EVENT REPORT (LER) 202672 FACAUTy NAMg til DOCFFT NUMBfB (2)
FACAUTy NAMg til                                                                                             DOCFFT NUMBfB (2)                     P AQf (3)
P AQf (3)
DIABLO CANYON UNIT 2                                                                               0l5l0l0l0l3l2l3                         1 l ' l 10 mu se ACCUMULATOR N0ZZLE CRACKING DUE TO INTERGRANULAR STRESS CORROSION EVENT DATE lli                             LEM NUMBEM IS)               REPOMT DATE tT)                           OTHER FACILIT]E$ INVOLVED (8)
DIABLO CANYON UNIT 2 0l5l0l0l0l3l2l3 1 l ' l 10 mu se ACCUMULATOR N0ZZLE CRACKING DUE TO INTERGRANULAR STRESS CORROSION EVENT DATE lli LEM NUMBEM IS)
MO21       DAY   YM       YR         SEQUENTIAL         REVlaAON   MON   DAY       YR                                       DOCKET NUM8ER 483 NtusEn           Nuuafn 0   5   0 0       0   2   7 5 l                                                                                               DIABLO CANYON UNIT 1
REPOMT DATE tT)
  ! 10 RA NG 09     87     87     -
OTHER FACILIT]E$ INVOLVED (8)
0l2l3           -
MO21 DAY YM YR SEQUENTIAL REVlaAON MON DAY YR DOCKET NUM8ER 483 NtusEn Nuuafn 0
0l1       02     01       93 TM15 REPORT !$ $UBMITTED PUR5UANT TO THE REQUIREMENT 5 0F to CFR 0    5  0  0      0 (11) 1 LNEY                                                     10 CFR 110l0                                 X     OTHER -           VOLUNTARY (Specify in Abstract below and in text, NRC Form 366A) uctNsEt cont AcT FoR Tus (En tiri j                                                                                                                                     TEttP e r aumero                   l l              DAVID P. SISK, SENIOR REGULATORY COMPLIANCE ENGINEER                                                         ^""c"'
5 0
805                     545-4420         ,
0 0
COMPLET s ONE UNE FOR EACH COMPONENT FAILURE DESCRIEED IN TMS MEPORT (13)                                                 1 CAU$C     $YSTEM   CCMPONENT       MANUFAC.       R O       E                     CAUSE   $T3 TEM     COMPONENT     MANUF AC.       R O       E I       III             III                                                         I       III           III I     lil               11I safufN T At atP RT LxPEcTEa si A3 I      lll          Ill    " "T"           D"'           'E^^
2 7
EXPECTED i                                                                                                             SUBMISSION l     l l YES (if yes, Complete EXPECTED SUBMISSION DATE)                                                       ^   (
5 l
lX l          NO A$$ TRACT (16) 1 This voluntary Licensee Event Report (LER) is submitted for information only as                                                                             I iscribed in Item 19 of Supplement Number 1 to NUREG-1022.
DIABLO CANYON UNIT 1
Revision 0 of this LER described leaks in Unit 2 accumulator nozzles resulting from intergranular stress corrosion cracking (IGSCC) and a weld defect. This revision of the LER reports cracking in both Units 1 and 2 accumulator nozzlu identified during planned refueling outage inspections as a result of using                                                                                 )
! 10 09 87 87 0l2l3 0l1 02 01 93 0
inspection techniques of higher sensitivity than those previously used.                                                                                     ,
5 0
l The root cause of the flaws identified was IGSCC caused by a combination of factors during manufacture of the accumulators and a suitable incubation time.
0 0
RA NG TM15 REPORT !$ $UBMITTED PUR5UANT TO THE REQUIREMENT 5 0F to CFR (11) 1 LNEY 10 CFR 110l0 X
OTHER -
VOLUNTARY (Specify in Abstract below and in text, NRC Form 366A) uctNsEt cont AcT FoR Tus (En tiri j
TEttP e r aumero l
DAVID P. SISK, SENIOR REGULATORY COMPLIANCE ENGINEER
^""c"'
805 545-4420 COMPLET s ONE UNE FOR EACH COMPONENT FAILURE DESCRIEED IN TMS MEPORT (13) 1 CAU$C
$YSTEM CCMPONENT MANUFAC.
R O E
CAUSE
$T3 TEM COMPONENT MANUF AC.
R O E
I III III I
III III I
lil 11I I
lll Ill safufN T At atP RT LxPEcTEa si A3 EXPECTED
" "T" D"'
'E^^
i SUBMISSION l
l l YES (if yes, Complete EXPECTED SUBMISSION DATE) lX l NO
^
(
A$$ TRACT (16)
This voluntary Licensee Event Report (LER) is submitted for information only as iscribed in Item 19 of Supplement Number 1 to NUREG-1022.
Revision 0 of this LER described leaks in Unit 2 accumulator nozzles resulting from intergranular stress corrosion cracking (IGSCC) and a weld defect.
This revision of the LER reports cracking in both Units 1 and 2 accumulator nozzlu identified during planned refueling outage inspections as a result of using inspection techniques of higher sensitivity than those previously used.
The root cause of the flaws identified was IGSCC caused by a combination of factors during manufacture of the accumulators and a suitable incubation time.
All identified flaws were repaired or the nozzles were replaced, as appropriate.
All identified flaws were repaired or the nozzles were replaced, as appropriate.
Attachments 1 and 2 provide a complete repair history of Units 1 and 2 accumulator nozzles.
Attachments 1 and 2 provide a complete repair history of Units 1 and 2 accumulator nozzles.
1091S/85K
1091S/85K


LICENSEE EVENT REPORT (LER) TEXT CONTINUATION                 202672 mmu - m                                           man -.a m
LICENSEE EVENT REPORT (LER) TEXT CONTINUATION 202672
_      u=m      _
~m u=m mmu - m man -.a m DIABLO CANYON UNIT 2 0l5l0l0l0l3l2l3 87
                                                                                              ~m DIABLO CANYON UNIT 2                         0l5l0l0l0l3l2l3 87   -
- 0l2l3 Oll 2 l'l10 mi(u) 1.
0l2l3 -
Plant Conditions Units 1 and 2 have been in various Modes and at various power levels with the identified flaws in existence.
Oll 2 l'l10 mi(u)
II.
: 1. Plant Conditions Units 1 and 2 have been in various Modes and at various power levels with the identified flaws in existence.                                                             ,
Descriotion of Event A.
Descriotion of Event II.
Event:
A. Event:
l From October 1985 until April 1987, Unit 2 had experienced several.
l             From October 1985 until April 1987, Unit 2 had experienced several.
very small leaks on the emergency core cooling system accumulator. tank (BP)(ACC) sample and fill line nozzles (BP)(NZL).
very small leaks on the emergency core cooling system accumulator. tank (BP)(ACC) sample and fill line nozzles (BP)(NZL). These leaks were all minor, resulting in only small deposits of boric acid precipitates. The leaks resulted from intergranular stress corrosion                     '
These leaks were all minor, resulting in only small deposits of boric acid precipitates. The leaks resulted from intergranular stress corrosion cracking (IGSCC) with the exception of.one leak which resulted from a weld defect introdt jed during manufactaring. All laaking nozzles were identified and successfully repaired or replaced, and surveillance j
cracking (IGSCC) with the exception of.one leak which resulted from a weld defect introdt jed during manufactaring. All laaking nozzles were identified and successfully repaired or replaced, and surveillance j             inspection frequency was increased.
inspection frequency was increased.
In November 1985, PG&E informed Westinghouse of leaking nozzles on Accumulators 2-1 and 2-3. Accumulator 2-1 was found to be leaking at the socket weld connection on the 4-inch diameter fill line nozzle (nozzle G). A visual and dye penetrant examination indicated that the.
In November 1985, PG&E informed Westinghouse of leaking nozzles on Accumulators 2-1 and 2-3.
leak was the result of lack of fusion between the socket weld and nozzle. This defect was removed and weld repaired. Accumulator 2-3 was found to be leaking at nozzle G above the socket weld connection.
Accumulator 2-1 was found to be leaking at the socket weld connection on the 4-inch diameter fill line nozzle (nozzle G).
Dye penetrant examination and investigative grinding revealed parallel longitudinal linear indications around the nozzle circumference. The-location of these indications precluded weld repair.and the defective portion of the nozzle was replaced. Data at that time indicated that the leakage was due to poor fabrication and the use of dissimilar                   --
A visual and dye penetrant examination indicated that the.
        ]             mJtal in the nozzle socket; IGSCC had not yet been cor-idered as'a possible cause.
leak was the result of lack of fusion between the socket weld and nozzle. This defect was removed and weld repaired.
In October 1986, Accumulators 2-2 and 2-4 experienced very small -leaks at the socket region of the 3/4-inch diameter sample line nozzles (nozzle D). No previous history of leaking had been noted on Accumulator 2-4; however, the nozzle on Accumulator 2-2 had previously leaked and had been weld repaired in February 1986.
Accumulator 2-3 was found to be leaking at nozzle G above the socket weld connection.
Dye penetrant examination and investigative grinding revealed parallel longitudinal linear indications around the nozzle circumference.
The-location of these indications precluded weld repair.and the defective portion of the nozzle was replaced.
Data at that time indicated that the leakage was due to poor fabrication and the use of dissimilar
]
mJtal in the nozzle socket; IGSCC had not yet been cor-idered as'a possible cause.
In October 1986, Accumulators 2-2 and 2-4 experienced very small -leaks at the socket region of the 3/4-inch diameter sample line nozzles (nozzle D).
No previous history of leaking had been noted on Accumulator 2-4; however, the nozzle on Accumulator 2-2 had previously leaked and had been weld repaired in February 1986.
During the Unit 2 first refueling outage (2RI), the D nozzles were removed from Accumulators 2-2 and 2-4 and a detailed metallurgical examination was performed to ascertain the root cause of the leaks.
During the Unit 2 first refueling outage (2RI), the D nozzles were removed from Accumulators 2-2 and 2-4 and a detailed metallurgical examination was performed to ascertain the root cause of the leaks.
Sensitization testing using ASTM A-262 Practice A was performed and both nozzles were found to have heavily sensitized microstructures.
Sensitization testing using ASTM A-262 Practice A was performed and both nozzles were found to have heavily sensitized microstructures.
IGSCC was found in the socket region of the nozzle D-from Accumulator 2-2. Crack propagation was from-the nozzle inside diameter to outside. Though no cracking.was found on Nozzle D from Accumulator 2-4, IGSCC was not ruled out because this leak was 1091S/85K                                                                                               l
IGSCC was found in the socket region of the nozzle D-from Accumulator 2-2.
                                  -=     --      . _ , - . . .            .                    _ . . _ .
Crack propagation was from-the nozzle inside diameter to outside. Though no cracking.was found on Nozzle D from Accumulator 2-4, IGSCC was not ruled out because this leak was 1091S/85K l
-=


  -          . __ =   -      -    -- .      .                        _ .-      .
__ =
LICENSEE EVENT REPORT (LER) TEXT CONTINUATION                         202672                   e FCCILIIV 06AME (1)                               DOCr(f NUM8( A (2)           LER BrJMeth fG)               PAGE (3)
LICENSEE EVENT REPORT (LER) TEXT CONTINUATION 202672 e
* vpa     na   at     as                       a tsar (37)
FCCILIIV 06AME (1)
DIABLO CANYON UNIT 2                     0l5l0l0l0l3l2l3       87 -
DOCr(f NUM8( A (2)
0l2l3       -
LER BrJMeth fG)
0 l1l 3 l*'l 10 extremely small, not easily detectable, and evidence of IGSCC may have been cut out when the nozzle was cut off the accumulator. Chemical analysis in the socket region of both nozzles indicated primarily sulfur and some chloride contamination'. Sulfur and chlorides were also found in the 2-2 IGSCC crack region. A design change was implemented to replace the socket weld nozzles with butt weld end (BWE) nozzles of Type 304L.
PAGE (3) vpa na at as a
DIABLO CANYON UNIT 2 0l5l0l0l0l3l2l3 87
- 0l2l3 0 l1l 3 l*'l 10 tsar (37) extremely small, not easily detectable, and evidence of IGSCC may have been cut out when the nozzle was cut off the accumulator.
Chemical analysis in the socket region of both nozzles indicated primarily sulfur and some chloride contamination'.
Sulfur and chlorides were also found in the 2-2 IGSCC crack region.
A design change was implemented to replace the socket weld nozzles with butt weld end (BWE) nozzles of Type 304L.
The accumulators were manufactured by Delta Southern of Baton Rouge, Louisiana, under Westinghouse Specification No. 676441, and supplied as part of the Nuclear Steam Supply System Contract Scope.
The accumulators were manufactured by Delta Southern of Baton Rouge, Louisiana, under Westinghouse Specification No. 676441, and supplied as part of the Nuclear Steam Supply System Contract Scope.
An investigation by Westinghouse determined that 38 Westinghouse NSSS-supplied plants have been supplied with accumulators from the same supplier (Delta Southern). Westinghouse had no evidence at that-time that the IGSCC observed at DCPP had been experienced by any of the i                           other utilities supplied with these vessels.
An investigation by Westinghouse determined that 38 Westinghouse NSSS-supplied plants have been supplied with accumulators from the same supplier (Delta Southern).
l l                           On January 30, 1991, NRC Information Notice No. 91-05, "Intergranular l                           Stress Corrosion Cracking in Pressurized Water-Reactor Safety l                           Injection Accumulator Nozzles," was issued. This Information Notice informed licensees of problems involving IGSCC of pressurized water reactor safety injection accumulator nozzles.
Westinghouse had no evidence at that-time that the IGSCC observed at DCPP had been experienced by any of the i
Prior to the Unit 2 fourth refueling outage (2R4), an ASME Code Case removed hydrostatic testing as a requirement for accumulator inspection. PG&E's Inservice Inspection (ISI) personnel performed a walkdown on September 1, 1991, with the system at normal pressure and found a small trace of boron at the Accumulator 2-2 nozzle C-B upper connection. A snoop test found no trace of an active leak.                                             I On September 2,1991, using high level magnification, traces of a linear indication were noted. Ultrasonic testing (UT) inspections were performed on accumulator couplings for indication of cracking.
other utilities supplied with these vessels.
l Indications of cracking were found on Accumulator 2-2 upper nozzle C-B. An action plan was generated to investigate the indications on Accumulator 2-2 and to additionally inspect other                                       i accumulator nozzles.
l l
On January 30, 1991, NRC Information Notice No. 91-05, "Intergranular l
Stress Corrosion Cracking in Pressurized Water-Reactor Safety l
Injection Accumulator Nozzles," was issued.
This Information Notice informed licensees of problems involving IGSCC of pressurized water reactor safety injection accumulator nozzles.
Prior to the Unit 2 fourth refueling outage (2R4), an ASME Code Case removed hydrostatic testing as a requirement for accumulator inspection.
PG&E's Inservice Inspection (ISI) personnel performed a walkdown on September 1, 1991, with the system at normal pressure and found a small trace of boron at the Accumulator 2-2 nozzle C-B upper connection.
A snoop test found no trace of an active leak.
On September 2,1991, using high level magnification, traces of a linear indication were noted. Ultrasonic testing (UT) inspections were performed on accumulator couplings for indication of cracking.
Indications of cracking were found on Accumulator 2-2 upper l
nozzle C-B.
An action plan was generated to investigate the indications on Accumulator 2-2 and to additionally inspect other i
accumulator nozzles.
Further inspections revealed indications on Accumulator 2-1 lower.
Further inspections revealed indications on Accumulator 2-1 lower.
nozzle C-A, Accumulator 2-3 skirt coupling G, and multiple indications                                 .
nozzle C-A, Accumulator 2-3 skirt coupling G, and multiple indications on Accumulator 2-3 bottom nozzle D.
l on Accumulator 2-3 bottom nozzle D.
On September 26, 1991, dye penetrant testing-(PT) found indications on Accumulator 2-1 interior weld-to-clad material transition area just below the nozzle C-B bore and in the nozzle bore.
On September 26, 1991, dye penetrant testing-(PT) found indications on Accumulator 2-1 interior weld-to-clad material transition area just below the nozzle C-B bore and in the nozzle bore. Grinding out the indications revealed significant cracks in the cladding down to'the base metal. PT of the weld-to-clad transition areas of the nozzles in all fcur Unit 2 accumulators was begun.
Grinding out the indications revealed significant cracks in the cladding down to'the base metal.
PT of the weld-to-clad transition areas of the nozzles in all fcur Unit 2 accumulators was begun.
10915/85K
10915/85K


I LICENSEE EVENT REPORT (LER) TEXT CONTINUATION                       202672 Lta musTR 1 6)         PAGE (3) 3 hcILITV hAME (a)                                  DOCKET NUM8ER (2) mean       muun DIABLO CANYON UNIT 2                     0l5l0l0l013l2l3       87 -
LICENSEE EVENT REPORT (LER) TEXT CONTINUATION 202672 hcILITV hAME (a)
0l2l3     -
DOCKET NUM8ER (2)
0l1 4 l'"l 10 TEAT (47)
Lta musTR 1 6)
On September 30, 1991, all Unit 2 pts were completed. Three                               l additional weld-to-clad transition areas were found to have                               i indications. The areas were adjacent to Accumulator 2-2 nozzle B,                         l Accumulator 2-3 nozzle A, and Accumulator 2-4 nozzle A. Nozzles A and                     !
PAGE (3) 3 mean muun DIABLO CANYON UNIT 2 0l5l0l0l013l2l3 87
B are in the upper head of the accumulators.                                             l All Unit 2 accumulator nozzles that had indications were replaced with 304L stainless steel nozzles, and all other indications found during the inspections were repaired during 2R4.                                                 ;
- 0l2l3 0l1 4 l'"l 10 TEAT (47)
On September 30, 1991, all Unit 2 pts were completed. Three additional weld-to-clad transition areas were found to have indications. The areas were adjacent to Accumulator 2-2 nozzle B, Accumulator 2-3 nozzle A, and Accumulator 2-4 nozzle A.
Nozzles A and B are in the upper head of the accumulators.
All Unit 2 accumulator nozzles that had indications were replaced with 304L stainless steel nozzles, and all other indications found during the inspections were repaired during 2R4.
On September 13, 1992, during planned Unit 1 UT of Accumulator 1-4, as part of the Unit 1 fifth refueling outage (IRS), unacceptable indications were identified in nozzle C-B, Cl-B and skirt coupling G.
On September 13, 1992, during planned Unit 1 UT of Accumulator 1-4, as part of the Unit 1 fifth refueling outage (IRS), unacceptable indications were identified in nozzle C-B, Cl-B and skirt coupling G.
These were replaced and the accumulator returned to service.
These were replaced and the accumulator returned to service.
B. Inoperable Structures, Components or Systems That Contributed               the Event:
B.
Inoperable Structures, Components or Systems That Contributed the Event:
None.
None.
C. Dates of Occurrences:
C.
: 1.     February 18, 1985:       Accumulator 2-2 nozzle D had linear indications. Nozzle D was weld repaired.
Dates of Occurrences:
: 2.     October 5, 1985:         Accumulator 2-1 nozzle G had linear indications. Nozzle G was weld repaired.
1.
                          ''      October 5, 1985:         Accumulator 2-3 nozzle G hailinear indications. Nozzle G was replaced.
February 18, 1985:
: 4.     October 29, 1986:       Accumulator 2-2 nozzle D was leaking.
Accumulator 2-2 nozzle D had linear indications. Nozzle D was weld repaired.
2.
October 5, 1985:
Accumulator 2-1 nozzle G had linear indications.
Nozzle G was weld repaired.
October 5, 1985:
Accumulator 2-3 nozzle G hailinear indications. Nozzle G was replaced.
4.
October 29, 1986:
Accumulator 2-2 nozzle D was leaking.
Nozzle D was replaced.
Nozzle D was replaced.
: 5.     October 29, 1986:         Accumulator 2-4 nozzle D was leaking.
5.
October 29, 1986:
Accumulator 2-4 nozzle D was leaking.
Nozzle D was replaced.
Nozzle D was replaced.
: 6. September 1, 1991:       Accumulator 2-2 nozzle C-B was leaking.
6.
Nozzle C-B was replaced. (See Attachment 2 for Unit 2 accumulator repair history.)
September 1, 1991:
I
Accumulator 2-2 nozzle C-B was leaking.
: 7. September 13, 1992:       Accumulator 1-4 nozzle C-B had an                       i indication. Nozzle C-B was repaired.                   !
Nozzle C-B was replaced.
(See for Unit 2 accumulator repair history.)
7.
September 13, 1992:
Accumulator 1-4 nozzle C-B had an indication.
Nozzle C-B was repaired.
(See Attachment 1 for Unit 1 accumulator repair history.)
(See Attachment 1 for Unit 1 accumulator repair history.)
                                                                                                                    )
)
1091S/85K
1091S/85K


I                                                                                                             i LICENSEE EVENT REPORT (LER) TEXT CONTINUATION                 2026'/2
I i
  ,murr = m                                         man   u m               ua =r. m           u.c m ma     maamm   navann
LICENSEE EVENT REPORT (LER) TEXT CONTINUATION 2026'/2
* l nn on DIABLO CANYON UNIT 2                         0l5l0l0l0l312l3     87 -
,murr = m man u m ua =r.
0l2l3 -
m u.c m ma maamm navann DIABLO CANYON UNIT 2 0l5l0l0l0l312l3 87 0l2l3 0 l1 5 l'l10 nn on D.
0 l1 5 l'l10     l D.       Other Systems or Secondary functions-Affected:
Other Systems or Secondary functions-Affected:
l I
I None.
None.
E.
E.       Method of Discovery:                                                                 !
Method of Discovery:
Small leaks were discovered at various times during visual examinations and system walkdowns. Planned inspections during refueling outages identif.ied additional nozzle cracking.
Small leaks were discovered at various times during visual examinations and system walkdowns.
F.       Operator Actions:
Planned inspections during refueling outages identif.ied additional nozzle cracking.
F.
Operator Actions:
l-l Not applicable.
l-l Not applicable.
G.       Safety System Responses:
G.
Safety System Responses:
None required.
None required.
III. Cause of Event                                                                                 l A.         Immediate Cause:
III. Cause of Event A.
The sample line nozzle (D) on Accumulators 2-2 and 2-4 leaked as a result of IGSCC. Fill line nozzle (G) on Accumulators 2-1 and 2-3 leaked. Accumulators 2-1 and 2-3 leaked as a result of lack of fusion               l between the socket weld and the nozzle and as a result of IGSCC,                     I respectively.
Immediate Cause:
Subsequent cracking identified with more sensitive inspection techniques was a result of IGSCC.                                                   ,
The sample line nozzle (D) on Accumulators 2-2 and 2-4 leaked as a result of IGSCC.
i B.       Root cause:                                                                         '
Fill line nozzle (G) on Accumulators 2-1 and 2-3 leaked. Accumulators 2-1 and 2-3 leaked as a result of lack of fusion between the socket weld and the nozzle and as a result of IGSCC, respectively.
Although the fill line nozzle samples from Accumulators 2-1 and 2-3     -
Subsequent cracking identified with more sensitive inspection techniques was a result of IGSCC.
are not available, based on the available evidence in 1987, the most probable cause of leakage for Accumulator 2-1 was a weld defect. For Accumulator 2-3 the most probable cause was IGSCC. This conclusion l                        was based on the dye penetrant and investigative grinding results which revealed parallel longitudinal linear indications like those of Accumulator 2-2. Metallographic examinations performed on nozzle D of Accumulators 2-2 and 2-4 revealed IGSCC on the Accumulator 2-2 nozzle.
i B.
Root cause:
Although the fill line nozzle samples from Accumulators 2-1 and 2-3 are not available, based on the available evidence in 1987, the most probable cause of leakage for Accumulator 2-1 was a weld defect.
For Accumulator 2-3 the most probable cause was IGSCC.
This conclusion was based on the dye penetrant and investigative grinding results l
which revealed parallel longitudinal linear indications like those of Accumulator 2-2.
Metallographic examinations performed on nozzle D of Accumulators 2-2 and 2-4 revealed IGSCC on the Accumulator 2-2 nozzle.
Review of manufacturing, installation, and operating records supportr.
Review of manufacturing, installation, and operating records supportr.
the conclusion that, with the exception of nozzle G on Accumulator 2-1, the Unit 2 sample and fill line nozzles ' leaked as a result of small base material intergranular stress corrosion cracks.
the conclusion that, with the exception of nozzle G on Accumulator 2-1, the Unit 2 sample and fill line nozzles ' leaked as a result of small base material intergranular stress corrosion cracks.
Cracking most likely was initiated because (1) sulfur and chloride contamination was present in the socket region _of the nozzles, (2) the 1091S/85K
Cracking most likely was initiated because (1) sulfur and chloride contamination was present in the socket region _of the nozzles, (2) the 1091S/85K


i l                             LICENSEE EVENT REPORT (LER) TEXT CONTINUATION                     2026'72
i l
\
LICENSEE EVENT REPORT (LER) TEXT CONTINUATION 2026'72
    ,Act u VV NAME (3)                                   DOCKET MJMBER (2)         (f8 NUMBER I8)       PAGE (3) l
\\
                                                                                ""      ",t'L"'   L"ll" DIABLO CANYON UNIT 2                       0l5l0l0l0l3l2l3       87 -
,Act u VV NAME (3)
0l2l3     -
DOCKET MJMBER (2)
0 l1 6 l 'l 10 1111 (a nozzles were highly sensitized, (3) the necessary aqueous environment was present, and (4) residual tensile stresses were present.
(f8 NUMBER I8)
PAGE (3) l
",t'L"'
L"ll" DIABLO CANYON UNIT 2 0l5l0l0l0l3l2l3 87
- 0l2l3 0 l1 6 l 'l 10 1111 (a nozzles were highly sensitized, (3) the necessary aqueous environment was present, and (4) residual tensile stresses were present.
The basis for this conclusion is:
The basis for this conclusion is:
: 1.     DCPP accumulators were supplied with the fill and sample lines between the vessel and skirt coupling installed by the vendor. Contaminants, most likely introduced as a result of fabrication (cutting oils, forming compounds, l                                 etc.) or contaminated hydrostatic testing water, were not I                                 removed during subsequent flushing because of the tight crevice between the pipe and the nozzle socket. Moreover, the tight controls on water chenistry at DCPP for hydrostatic testing, startup flushing, and accumulator inventory praclude the introduction of contaminants l                                  subsequent to manufacture.
1.
: 2.     The austenitic stainless steel nozzles were type 304 (i.e., not a low carbon grade) and were welded into the
DCPP accumulators were supplied with the fill and sample lines between the vessel and skirt coupling installed by the vendor.
                                - vessel prior to vessel post weld stress relief heat treatment.     Consequently, the nozzles underwent a heat treatment during stress relieving that would cause significant sensitization (carbide precipitation at the grain boundarias).
Contaminants, most likely introduced as a result of fabrication (cutting oils, forming compounds, l
: 3.     Sensitized type 304 stainless steel in stagnant 2000 ppm borated water systems at room temperature has been shown to be highly susceptible to IGSCC in the presence of trace amounts of chlorides and sulfur oxyanions. The primary contaminant identified was sulfur, along with some chlorides.
etc.) or contaminated hydrostatic testing water, were not I
: 4.       High local residual tensile stresses were present. These stresses were yield-stress-magnitude and were sufficient to initiate 1GSCC given the conditions of contaminates and sensitized structure. The stresses resulted from differential contraction between the stainless steel nozzle and the carbon steel vessel during cooling (nozzle to vessel welds; vessel was stress-relieved with nozzles in place) and from solidification and shrinkage stresses from welding (socket welds).
removed during subsequent flushing because of the tight crevice between the pipe and the nozzle socket.
: 5.       The orientation of the identifiable indications responsible for leakage were longitudinal for all leaks except for nozzle G on Accumulator 2-1. In that case, the leak is believed to have been caused by a weld defect (lack of fusion); in addition, the orientation was circumferential. Unlike the leaks for the D nozzles on Accumulators 2-2 and 2-4, there was no recurrence of 1091S/85K
: Moreover, the tight controls on water chenistry at DCPP for hydrostatic testing, startup flushing, and accumulator inventory praclude the introduction of contaminants subsequent to manufacture.
l 2.
The austenitic stainless steel nozzles were type 304 (i.e., not a low carbon grade) and were welded into the
- vessel prior to vessel post weld stress relief heat treatment.
Consequently, the nozzles underwent a heat treatment during stress relieving that would cause significant sensitization (carbide precipitation at the grain boundarias).
3.
Sensitized type 304 stainless steel in stagnant 2000 ppm borated water systems at room temperature has been shown to be highly susceptible to IGSCC in the presence of trace amounts of chlorides and sulfur oxyanions.
The primary contaminant identified was sulfur, along with some chlorides.
4.
High local residual tensile stresses were present.
These stresses were yield-stress-magnitude and were sufficient to initiate 1GSCC given the conditions of contaminates and sensitized structure. The stresses resulted from differential contraction between the stainless steel nozzle and the carbon steel vessel during cooling (nozzle to vessel welds; vessel was stress-relieved with nozzles in place) and from solidification and shrinkage stresses from welding (socket welds).
5.
The orientation of the identifiable indications responsible for leakage were longitudinal for all leaks except for nozzle G on Accumulator 2-1.
In that case, the leak is believed to have been caused by a weld defect (lack of fusion); in addition, the orientation was circumferential. Unlike the leaks for the D nozzles on Accumulators 2-2 and 2-4, there was no recurrence of 1091S/85K


LICENSEE EVENT REPORT (LER) TEXT CONTINUATION                   2()2672               i FAC3L3tv NAME (1)                                     DoCKEI NUMSER (2)         L(R NUMOfR 6)       D Ar.f (3)
LICENSEE EVENT REPORT (LER) TEXT CONTINUATION 2()2672 i
                                                                          ~                    """
FAC3L3tv NAME (1)
                                                                                  "K"             -
DoCKEI NUMSER (2)
TEXT (17)
L(R NUMOfR 6)
DIABLO CANYON UNIT 2                       0l5l0l0l0l3l2l3     87 -
D Ar.f (3)
0l2l3   -
"K"
0l1 7 l 'l 10 leakage after weld repair.                                                         i
~
: 6. With the exception of the nozzle G leak identified above, leaks that were initially stopped after being repaired with weld metal leaked again seven months following repair.
DIABLO CANYON UNIT 2 0l5l0l0l0l3l2l3 87
IV.     Analysis of Event The sample and fill lines are anchored to the accumulator nozzles and skirt, forming a stiff piping segment. Seismic loads would be expected to be low due to this stiff configuration, the anticipated response spectra, and no relative seismic displacement between the skirt and vessel nozzle. Thermal stresses are negligible because the service temperature of the accumulator inventory is essentially at containment ambient temperature. The applied-stress at the IGSCC location will, therefore, be primarily the result of pressure stress and should not exceed approximately 1500 psi tension and 870 psi shear. Accordingly, self-limiting _ residual stresses, rather than applied loads, contribute to crack initiation. Defect propagation beyond the shoulder region of the socket was not likely to occur as substantiated by the characteristics of the leaks observed and the very low service stresses.
- 0l2l3 0l1 7 l 'l 10 TEXT (17) leakage after weld repair.
Joint loads due to accumulator internal pressure are significantly less than                     !
i 6.
the expected shear capacity of the socket and neither defect propagation nor                     l catastrophic failure (separation of pipe and nozzle) would be expected as                         i the result of applied loads. The consequences of the defect going undetected would be limited to a continued very small leak. Early detection of a drop in accumulator level and/or pressure is provided by two channels for level detection and alarms. It is concluded that the leaks and-nsociated defects would not preclude delivery of sufficient accumulator inventory to the reactor coolant system. The accumulators would continue to perform their intended safety function.
With the exception of the nozzle G leak identified above, leaks that were initially stopped after being repaired with weld metal leaked again seven months following repair.
IV.
Analysis of Event The sample and fill lines are anchored to the accumulator nozzles and skirt, forming a stiff piping segment.
Seismic loads would be expected to be low due to this stiff configuration, the anticipated response spectra, and no relative seismic displacement between the skirt and vessel nozzle.
Thermal stresses are negligible because the service temperature of the accumulator inventory is essentially at containment ambient temperature.
The applied-stress at the IGSCC location will, therefore, be primarily the result of pressure stress and should not exceed approximately 1500 psi tension and 870 psi shear. Accordingly, self-limiting _ residual stresses, rather than applied loads, contribute to crack initiation.
Defect propagation beyond the shoulder region of the socket was not likely to occur as substantiated by the characteristics of the leaks observed and the very low service stresses.
Joint loads due to accumulator internal pressure are significantly less than the expected shear capacity of the socket and neither defect propagation nor catastrophic failure (separation of pipe and nozzle) would be expected as i
the result of applied loads.
The consequences of the defect going undetected would be limited to a continued very small leak.
Early detection of a drop in accumulator level and/or pressure is provided by two channels for level detection and alarms.
It is concluded that the leaks and-nsociated defects would not preclude delivery of sufficient accumulator inventory to the reactor coolant system.
The accumulators would continue to perform their intended safety function.
Therefore, there were no adverse safety consequences or implications
Therefore, there were no adverse safety consequences or implications
    }           resulting from this condition.
}
V.       Corrective Actions The leaking nozzle D on Accumulators 2-2 and 2-4 have been redesigned and replaced. The new design utilizes a butt welded connection and type 304L base material. The defective weld (lack of fusion) on nozzle G of Accumulator 2-1 has been weld repaired with no subsequent leakage. The leaking nozzle G on Accumulator 2-3 was repaired by replacement of defective-nozzle material.
resulting from this condition.
V.
Corrective Actions The leaking nozzle D on Accumulators 2-2 and 2-4 have been redesigned and replaced. The new design utilizes a butt welded connection and type 304L base material. The defective weld (lack of fusion) on nozzle G of Accumulator 2-1 has been weld repaired with no subsequent leakage.
The leaking nozzle G on Accumulator 2-3 was repaired by replacement of defective-nozzle material.
Attachments 1 and 2 summarize repairs performed un Units 1 and 2 accumulator nozzles during the IRS-and 2R4 refueling outages, respectively.
Attachments 1 and 2 summarize repairs performed un Units 1 and 2 accumulator nozzles during the IRS-and 2R4 refueling outages, respectively.
1091S/85K
1091S/85K


LICENSEE EVENT REPORT (LER) TEXT CONTINUATION               202672.
LICENSEE EVENT REPORT (LER) TEXT CONTINUATION 202672.
m             u.-t.,           nu o>
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j           DIABLO CANYON UNIT 2                   0l5l0l0l0l3l2l3     87 -
=. ~
0l2l3   -
=
0l1 8 l"l 10 itat (p)
j DIABLO CANYON UNIT 2 0l5l0l0l0l3l2l3 87
An enhanced periodic inspection program for accumulator nozzles is being developed and will be performed during future refueling outages.
- 0l2l3 0l1 8 l"l 10 itat (p) i An enhanced periodic inspection program for accumulator nozzles is being developed and will be performed during future refueling outages.
VI. Additional Information A. Accumulator tank data:
VI.
Manufacturer      -
Additional Information A.
Delta Southern Vendor           -    Westinghouse Material          -      Carbon steel, with 304 stainless steel liner -
Accumulator tank data:
Size              -
Delta Southern Manufacturer Westinghouse Vendor Carbon steel, with 304 stainless steel liner -
1350 cubic feet B. Previous LERs on similar events:
Material 1350 cubic feet Size B.
Previous LERs on similar events:
None.
None.
C. Attachments:
C.
: 1. Accumulator Nozzle Repair - Unit 1-
Attachments:
: 2. Accumulator Nozzle Repair - Unit 2 1
1.
                                                                                  .ev, l
Accumulator Nozzle Repair - Unit 1-2.
Accumulator Nozzle Repair - Unit 2
.ev, l
1091S/85K
 
LICENSEE EVENT REPORT (LER) TEXT CONTINUATION 202672
,m a,, - m mu, -u. m u. --.
ou m -
un" wuSu DIABLO CANYON UNIT 2 0l5l0l0l0l3l2l3 87 Ol2l3 0l1 9 l 'l 10 TEXT (37)
ATTACHMENT 1 ACCUMULATOR NOZZLE REPAIR - UNIT 1 ACCUMU-NOZZLE CARBON REPAIR TEST LATOR CONTENT HISTORY HISTORY I
1-1 A
.05 NONE NRI 1-1 B
.05 NONE NRI 1-1 C-A
.028 NONE NRI 1-1 C-B
.028 NONE NRI 1-1 C-1A
.028 NONE NRI 1-1 C-13
.028 NONE NRI 1-1 D
004 NONE NRI 1-1 E
NONE NRI 1-1 G
.05 NONE NRI 1-2 A
.05 NONE NRI 1-2 B
.05 NONE NRI l
1-2 C-A
.027 NONE NRI 1-2 C-B
.027 NONE NRI 1-2 C-1A
.027 NONE NRI 1-2 C-1B
.027 NONE NRI 1-2 D
004 NONE NRI 4
1-2 E
BUFFED 1-IND 1-2 G
.05 NONE NRI 1-3 A
.05 NONE NRI 1-3 B
.03 NONE NRI 1-3 C-A
.047 NONE NRI 1-3 C-B
.047 NONE NRI 1-3 C-1A
.047 NONE NRI 1-3 C-1B
.047 NONE NRI 1-3 D
.004 NONE NRI 1-3 E
.024 NONE NRI 1-3 G
.03 NONE NRI 1-4 A
.05 NONE NRI 1-4 B
.03 NONE NRI l-4 C-A
.0473 NONE NRI 3
1-4 C-B
.047 REPLACED 2-IND 1-4 C-1A
.0473 NONE NRI 3
1-4 C-1B
.047 REPLACED 3-IND 1-4 D
.004 NONE NRI 1-4 E
.024 NONE NRI 1-4 G
.03 REPAIRED ROUNDED IND 1-4 G (skirt cpl)
REPLACED 1-IND l
l l
l l
1091S/85K                                                                                       I
I No recordable indications l
2 Recorded data believed to be for F nozzle instead of E nozzle and, therefore, data may be in error.
l 3
Questionable or illegible 1091S/85K


LICENSEE EVENT REPORT (LER) TEXT CONTINUATION                         202672        *
202672 LICENSEE EVENT REPORT (LER) TEXT CONTINUATION c
  ,m a ,, - m                                          mu, -u. m                    u . -- . .>      ou m -
FACIL3f f hAME (3)
un"    wuSu TEXT (37)
DOCECT NUMBER (2)
DIABLO CANYON UNIT 2                      0l5l0l0l0l3l2l3        87  -
LES NUMBER 6)
Ol2l3  -
PAGE (3) 1 naR maamm Reveun.
0l1 9 l 'l 10 ATTACHMENT 1 ACCUMULATOR NOZZLE REPAIR - UNIT 1 ACCUMU-      NOZZLE        CARBON        REPAIR      TEST LATOR                      CONTENT        HISTORY    HISTORY
NUMER ORJMMR DIABLO CANYON UNIT 2 0l5l0l0l0l3l2l3 87 Ol2l3 0 l1 10 l 'l 10 TEXT (17)
_-----------------------------------------------------                                    l 1-1          A              .05          NONE        NRI I 1-1          B              .05          NONE        NRI 1-1          C-A            .028          NONE        NRI 1-1          C-B            .028          NONE        NRI 1-1          C-1A          .028          NONE        NRI 1-1          C-13          .028          NONE        NRI 1-1          D              004          NONE        NRI 1-1          E                          NONE          NRI 1-1          G              .05          NONE        NRI 1-2          A              .05          NONE        NRI 1-2          B              .05          NONE        NRI                                l 1-2          C-A            .027          NONE        NRI 1-2          C-B            .027        NONE          NRI 1-2          C-1A          .027          NONE        NRI 1-2          C-1B          .027          NONE        NRI 1-2          D              004        NONE          NRI 4
ATTACHMENT 2 ACCUMULATOR NOZZLE REPAIR - UNIT 2 ACCUMU-NOZZLE CARBON REPAIR TEST LATOR CONTENT HISTORY HISTORY I
1-2          E
2 2-1 A
* BUFFED        1-IND 1-2          G              .05          NONE          NRI 1-3          A            .05          NONE          NRI 1-3          B            .03          NONE          NRI 1-3          C-A          .047          NONE          NRI 1-3          C-B          .047          NONE          NRI 1-3          C-1A          .047          NONE          NRI 1-3          C-1B          .047          NONE          NRI 1-3          D            .004          NONE          NRI 1-3          E            .024          NONE          NRI 1-3          G            .03          NONE          NRI 1-4          A            .05          NONE          NRI 1-4          B            .03          NONE          NRI l-4          C-A          .0473        NONE          NRI 1-4          C-B          .047 3        REPLACED      2-IND 1-4          C-1A          .0473        NONE          NRI 1-4          C-1B          .047 3        REPLACED      3-IND 1-4          D            .004          NONE          NRI 1-4          E            .024          NONE          NRI 1-4          G            .03        REPAIRED ROUNDED IND 1-4          G (skirt cpl)              REPLACED      1-IND l
NONE NRI I
l I
2-1 B
l              No recordable indications 2
NONE NRI 1-IND 2-1 C-A
l
.05 gEPLACED 2-1 C-B
'                      Recorded data believed to be for F nozzle instead of E nozzle and, therefore, data may be in error.
.05 NRI 2-1 C-1A
3 l              Questionable or illegible 1091S/85K
.05 NONE NRI 2-1 C-1B
 
.05 NONE NRI4 2-1 D
202672                    l c
.05 NONE NRI 2-1 E
LICENSEE EVENT REPORT (LER) TEXT CONTINUATION                                                                    !
061 NONE NDI I
FACIL3f f hAME (3)                                           DOCECT NUMBER (2)                         LES NUMBER 1
4 2-1 G
: 6)         PAGE (3) naR       maamm       Reveun.
REPAIRED NRI 2-2 A
NUMER       ORJMMR DIABLO CANYON UNIT 2                               0l5l0l0l0l3l2l3                   87   -
.04 NONE NRI 2-2 B
Ol2l3       -
.04 REPAIRED 1-IND 2-2 C-A
0 l1   10 l 'l 10 !
.05 NONE NRI 2-2 C-B
TEXT (17)
.05 REPLACED 3-IND 2-2 C-1A
ATTACHMENT 2 ACCUMULATOR NOZZLE REPAIR - UNIT 2 ACCUMU-             NOZZLE       CARBON             REPAIR               TEST LATOR                           CONTENT             HISTORY             HISTORY 2-1                 A           I                  NONE                 NRI 2 2-1                 B I                  NONE                 NRI 2-1                 C-A         .05                 gEPLACED             1-IND 2-1                 C-B         .05                                       NRI 2-1                 C-1A         .05                 NONE                 NRI 2-1                 C-1B         .05                 NONE                 NRI 2-1                 D           .05                 NONE                 NRI 4 2-1                 E               061             NONE                 NDI 2-1                 G           I                  REPAIRED             NRI 4 2-2                 A           .04                 NONE                 NRI 2-2                 B           .04                 REPAIRED             1-IND 2-2                 C-A         .05                 NONE                 NRI 2-2                 C-B         .05                 REPLACED             3-IND 2-2                 C-1A         .05               NONE                 NRI 2-2                 C-1B         .05               NONE                 NRI 2-2                 D             .05               REPLACED             NRI 4 2-2                 E             .061               NONE                 NRI 2-2                 G             .053               NONE                 NRI 4 2-3                 A             .04               REPAIRED             1-IND 2-3                 B             .04               NONE                 NRI 2-3                 C-A           .05               NONE                 NRI 2-3                 C-B           .05               NONE                 NRI 2-3                 C-1A         .05               REPAIRED             NRI 2-3                 C-1B         .05               REPAIRED             NRI 2-3                 D             .05               REPLACED             2-IND
.05 NONE NRI 2-2 C-1B
                          .m2-3                 E             .061               NONE                 NRI;"
.05 NONE NRI4 2-2 D
2-3                 G             .04               NONE                 NRI 2-3                 G (skirt cpl)                   REPLACED             1-IND                                   l l
.05 REPLACED NRI 2-2 E
2-4                 A             .04               REPAIRED             1-IND 2-4                 B             .04               NONE                 NRI' 2-4                 C-A           .05               NONE                 NRI 2-4                 C-B           .05               NONE                 NRI 2-4                 C-1A         .05               NONE                 NRI 2-4                 C-1B         .05               NONE                 NRI 2-4                 D             . 0 5-             REPLACED             NRI I 2-4                 E             .061               NONE                 NRI 2-4                 G             .04               NONE               , NRI 4 i
.061 NONE NRI4 2-2 G
.053 NONE NRI 2-3 A
.04 REPAIRED 1-IND 2-3 B
.04 NONE NRI 2-3 C-A
.05 NONE NRI 2-3 C-B
.05 NONE NRI 2-3 C-1A
.05 REPAIRED NRI 2-3 C-1B
.05 REPAIRED NRI 2-3 D
.05 REPLACED 2-IND
.m2-3 E
.061 NONE NRI;"
2-3 G
.04 NONE NRI 2-3 G (skirt cpl)
REPLACED 1-IND l
2-4 A
.04 REPAIRED 1-IND 2-4 B
.04 NONE NRI' 2-4 C-A
.05 NONE NRI 2-4 C-B
.05 NONE NRI 2-4 C-1A
.05 NONE NRI 2-4 C-1B
.05 NONE NRI I 2-4 D
. 0 5-REPLACED NRI 2-4 E
.061 NONE NRI 4 2-4 G
.04 NONE
, NRI i
l l
l I
l I
l          l                Questionable or illegible 2
Questionable or illegible l
l                No recordable indications 3
2 No recordable indications 3
l               Linear indication in 1985.               Accepted-as-is.
l Linear indication in 1985.
4 Limited examination due to bottom curvature.                                 Generally, only 1800 scanned.
Accepted-as-is.
4 0
Limited examination due to bottom curvature.
Generally, only 180 scanned.
1091S/85K}}
1091S/85K}}

Latest revision as of 22:22, 16 December 2024

Intervenor Exhibit I-MFP-60,consisting of LER 2-87-023-01, Re Dockets 50-275 & 50-323,dtd 930201
ML20062M715
Person / Time
Site: Diablo Canyon  Pacific Gas & Electric icon.png
Issue date: 08/18/1993
From: Rueger G
PACIFIC GAS & ELECTRIC CO.
To:
References
OLA-2-I-MFP-060, OLA-2-I-MFP-60, NUDOCS 9401110149
Download: ML20062M715 (11)


Text

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6-295lnep 46 323 OAL rze.

r.- i Pacific Gas and Electric Company 77 Bea!e Street Gregory M. Rueger 6enior Vice President and San Francisco.CA 94106 r~r# q/c" General Manager

's 415/973-4684 t

Nuclear Power Generation l

l 73 C M N ?

February 1, 1993 PG&E Letter No. DCL-93-026 U.S. Nuclear Regulatory Commission ATTN:

Document Control Desk Washington, D.C.

20555 Re:

Docket No. 50-275, OL-DPR-80 Docket No. 50-323, OL-DPR-82 Diablo Canyon Units 1 and 2 Licensee Event Report 2-87-023-01 (Voluntary)

Accumulator Nozzle Cracking Due to Intergranular Stress Corrosion Gentlemen:

PG&E is submitting a revision to voluntary Licensee Event Report 2-87-023-00 concerning intergranular stress corrosion cracking in bah Units 1 and 2 accumulator nozzles.

This revision is submitted to report the results of inspections and repair actions performed during the Unit 2 fourth refueling outage and the Unit 1 fifth refueling outage.

This report is submitted for information purposes only as described in Item 19 of supplement I to NUREG-1022.

Revision bars in the margin indicate the revised LER sections.

This event has in no way affected the health and safety of the public.

Sincerely,

'M AW

.c Gregory M. Rueger cc:

Ann P. Hodgdon John B. Martin Mary H. Miller Sheri R. Peterson CPUC Diablo Distribution INP0 taucttAn Rtcui Aron cov:.tesion

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9401110149 930818 PDR ADDCK 05000275 O

PDR

l' LICENSEE EVENT REPORT (LER) 202672 FACAUTy NAMg til DOCFFT NUMBfB (2)

P AQf (3)

DIABLO CANYON UNIT 2 0l5l0l0l0l3l2l3 1 l ' l 10 mu se ACCUMULATOR N0ZZLE CRACKING DUE TO INTERGRANULAR STRESS CORROSION EVENT DATE lli LEM NUMBEM IS)

REPOMT DATE tT)

OTHER FACILIT]E$ INVOLVED (8)

MO21 DAY YM YR SEQUENTIAL REVlaAON MON DAY YR DOCKET NUM8ER 483 NtusEn Nuuafn 0

5 0

0 0

2 7

5 l

DIABLO CANYON UNIT 1

! 10 09 87 87 0l2l3 0l1 02 01 93 0

5 0

0 0

RA NG TM15 REPORT !$ $UBMITTED PUR5UANT TO THE REQUIREMENT 5 0F to CFR (11) 1 LNEY 10 CFR 110l0 X

OTHER -

VOLUNTARY (Specify in Abstract below and in text, NRC Form 366A) uctNsEt cont AcT FoR Tus (En tiri j

TEttP e r aumero l

DAVID P. SISK, SENIOR REGULATORY COMPLIANCE ENGINEER

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805 545-4420 COMPLET s ONE UNE FOR EACH COMPONENT FAILURE DESCRIEED IN TMS MEPORT (13) 1 CAU$C

$YSTEM CCMPONENT MANUFAC.

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A$$ TRACT (16)

This voluntary Licensee Event Report (LER) is submitted for information only as iscribed in Item 19 of Supplement Number 1 to NUREG-1022.

Revision 0 of this LER described leaks in Unit 2 accumulator nozzles resulting from intergranular stress corrosion cracking (IGSCC) and a weld defect.

This revision of the LER reports cracking in both Units 1 and 2 accumulator nozzlu identified during planned refueling outage inspections as a result of using inspection techniques of higher sensitivity than those previously used.

The root cause of the flaws identified was IGSCC caused by a combination of factors during manufacture of the accumulators and a suitable incubation time.

All identified flaws were repaired or the nozzles were replaced, as appropriate.

Attachments 1 and 2 provide a complete repair history of Units 1 and 2 accumulator nozzles.

1091S/85K

LICENSEE EVENT REPORT (LER) TEXT CONTINUATION 202672

~m u=m mmu - m man -.a m DIABLO CANYON UNIT 2 0l5l0l0l0l3l2l3 87

- 0l2l3 Oll 2 l'l10 mi(u) 1.

Plant Conditions Units 1 and 2 have been in various Modes and at various power levels with the identified flaws in existence.

II.

Descriotion of Event A.

Event:

l From October 1985 until April 1987, Unit 2 had experienced several.

very small leaks on the emergency core cooling system accumulator. tank (BP)(ACC) sample and fill line nozzles (BP)(NZL).

These leaks were all minor, resulting in only small deposits of boric acid precipitates. The leaks resulted from intergranular stress corrosion cracking (IGSCC) with the exception of.one leak which resulted from a weld defect introdt jed during manufactaring. All laaking nozzles were identified and successfully repaired or replaced, and surveillance j

inspection frequency was increased.

In November 1985, PG&E informed Westinghouse of leaking nozzles on Accumulators 2-1 and 2-3.

Accumulator 2-1 was found to be leaking at the socket weld connection on the 4-inch diameter fill line nozzle (nozzle G).

A visual and dye penetrant examination indicated that the.

leak was the result of lack of fusion between the socket weld and nozzle. This defect was removed and weld repaired.

Accumulator 2-3 was found to be leaking at nozzle G above the socket weld connection.

Dye penetrant examination and investigative grinding revealed parallel longitudinal linear indications around the nozzle circumference.

The-location of these indications precluded weld repair.and the defective portion of the nozzle was replaced.

Data at that time indicated that the leakage was due to poor fabrication and the use of dissimilar

]

mJtal in the nozzle socket; IGSCC had not yet been cor-idered as'a possible cause.

In October 1986, Accumulators 2-2 and 2-4 experienced very small -leaks at the socket region of the 3/4-inch diameter sample line nozzles (nozzle D).

No previous history of leaking had been noted on Accumulator 2-4; however, the nozzle on Accumulator 2-2 had previously leaked and had been weld repaired in February 1986.

During the Unit 2 first refueling outage (2RI), the D nozzles were removed from Accumulators 2-2 and 2-4 and a detailed metallurgical examination was performed to ascertain the root cause of the leaks.

Sensitization testing using ASTM A-262 Practice A was performed and both nozzles were found to have heavily sensitized microstructures.

IGSCC was found in the socket region of the nozzle D-from Accumulator 2-2.

Crack propagation was from-the nozzle inside diameter to outside. Though no cracking.was found on Nozzle D from Accumulator 2-4, IGSCC was not ruled out because this leak was 1091S/85K l

-=

__ =

LICENSEE EVENT REPORT (LER) TEXT CONTINUATION 202672 e

FCCILIIV 06AME (1)

DOCr(f NUM8( A (2)

LER BrJMeth fG)

PAGE (3) vpa na at as a

DIABLO CANYON UNIT 2 0l5l0l0l0l3l2l3 87

- 0l2l3 0 l1l 3 l*'l 10 tsar (37) extremely small, not easily detectable, and evidence of IGSCC may have been cut out when the nozzle was cut off the accumulator.

Chemical analysis in the socket region of both nozzles indicated primarily sulfur and some chloride contamination'.

Sulfur and chlorides were also found in the 2-2 IGSCC crack region.

A design change was implemented to replace the socket weld nozzles with butt weld end (BWE) nozzles of Type 304L.

The accumulators were manufactured by Delta Southern of Baton Rouge, Louisiana, under Westinghouse Specification No. 676441, and supplied as part of the Nuclear Steam Supply System Contract Scope.

An investigation by Westinghouse determined that 38 Westinghouse NSSS-supplied plants have been supplied with accumulators from the same supplier (Delta Southern).

Westinghouse had no evidence at that-time that the IGSCC observed at DCPP had been experienced by any of the i

other utilities supplied with these vessels.

l l

On January 30, 1991, NRC Information Notice No. 91-05, "Intergranular l

Stress Corrosion Cracking in Pressurized Water-Reactor Safety l

Injection Accumulator Nozzles," was issued.

This Information Notice informed licensees of problems involving IGSCC of pressurized water reactor safety injection accumulator nozzles.

Prior to the Unit 2 fourth refueling outage (2R4), an ASME Code Case removed hydrostatic testing as a requirement for accumulator inspection.

PG&E's Inservice Inspection (ISI) personnel performed a walkdown on September 1, 1991, with the system at normal pressure and found a small trace of boron at the Accumulator 2-2 nozzle C-B upper connection.

A snoop test found no trace of an active leak.

On September 2,1991, using high level magnification, traces of a linear indication were noted. Ultrasonic testing (UT) inspections were performed on accumulator couplings for indication of cracking.

Indications of cracking were found on Accumulator 2-2 upper l

nozzle C-B.

An action plan was generated to investigate the indications on Accumulator 2-2 and to additionally inspect other i

accumulator nozzles.

Further inspections revealed indications on Accumulator 2-1 lower.

nozzle C-A, Accumulator 2-3 skirt coupling G, and multiple indications on Accumulator 2-3 bottom nozzle D.

On September 26, 1991, dye penetrant testing-(PT) found indications on Accumulator 2-1 interior weld-to-clad material transition area just below the nozzle C-B bore and in the nozzle bore.

Grinding out the indications revealed significant cracks in the cladding down to'the base metal.

PT of the weld-to-clad transition areas of the nozzles in all fcur Unit 2 accumulators was begun.

10915/85K

LICENSEE EVENT REPORT (LER) TEXT CONTINUATION 202672 hcILITV hAME (a)

DOCKET NUM8ER (2)

Lta musTR 1 6)

PAGE (3) 3 mean muun DIABLO CANYON UNIT 2 0l5l0l0l013l2l3 87

- 0l2l3 0l1 4 l'"l 10 TEAT (47)

On September 30, 1991, all Unit 2 pts were completed. Three additional weld-to-clad transition areas were found to have indications. The areas were adjacent to Accumulator 2-2 nozzle B, Accumulator 2-3 nozzle A, and Accumulator 2-4 nozzle A.

Nozzles A and B are in the upper head of the accumulators.

All Unit 2 accumulator nozzles that had indications were replaced with 304L stainless steel nozzles, and all other indications found during the inspections were repaired during 2R4.

On September 13, 1992, during planned Unit 1 UT of Accumulator 1-4, as part of the Unit 1 fifth refueling outage (IRS), unacceptable indications were identified in nozzle C-B, Cl-B and skirt coupling G.

These were replaced and the accumulator returned to service.

B.

Inoperable Structures, Components or Systems That Contributed the Event:

None.

C.

Dates of Occurrences:

1.

February 18, 1985:

Accumulator 2-2 nozzle D had linear indications. Nozzle D was weld repaired.

2.

October 5, 1985:

Accumulator 2-1 nozzle G had linear indications.

Nozzle G was weld repaired.

October 5, 1985:

Accumulator 2-3 nozzle G hailinear indications. Nozzle G was replaced.

4.

October 29, 1986:

Accumulator 2-2 nozzle D was leaking.

Nozzle D was replaced.

5.

October 29, 1986:

Accumulator 2-4 nozzle D was leaking.

Nozzle D was replaced.

6.

September 1, 1991:

Accumulator 2-2 nozzle C-B was leaking.

Nozzle C-B was replaced.

(See for Unit 2 accumulator repair history.)

7.

September 13, 1992:

Accumulator 1-4 nozzle C-B had an indication.

Nozzle C-B was repaired.

(See Attachment 1 for Unit 1 accumulator repair history.)

)

1091S/85K

I i

LICENSEE EVENT REPORT (LER) TEXT CONTINUATION 2026'/2

,murr = m man u m ua =r.

m u.c m ma maamm navann DIABLO CANYON UNIT 2 0l5l0l0l0l312l3 87 0l2l3 0 l1 5 l'l10 nn on D.

Other Systems or Secondary functions-Affected:

I None.

E.

Method of Discovery:

Small leaks were discovered at various times during visual examinations and system walkdowns.

Planned inspections during refueling outages identif.ied additional nozzle cracking.

F.

Operator Actions:

l-l Not applicable.

G.

Safety System Responses:

None required.

III. Cause of Event A.

Immediate Cause:

The sample line nozzle (D) on Accumulators 2-2 and 2-4 leaked as a result of IGSCC.

Fill line nozzle (G) on Accumulators 2-1 and 2-3 leaked. Accumulators 2-1 and 2-3 leaked as a result of lack of fusion between the socket weld and the nozzle and as a result of IGSCC, respectively.

Subsequent cracking identified with more sensitive inspection techniques was a result of IGSCC.

i B.

Root cause:

Although the fill line nozzle samples from Accumulators 2-1 and 2-3 are not available, based on the available evidence in 1987, the most probable cause of leakage for Accumulator 2-1 was a weld defect.

For Accumulator 2-3 the most probable cause was IGSCC.

This conclusion was based on the dye penetrant and investigative grinding results l

which revealed parallel longitudinal linear indications like those of Accumulator 2-2.

Metallographic examinations performed on nozzle D of Accumulators 2-2 and 2-4 revealed IGSCC on the Accumulator 2-2 nozzle.

Review of manufacturing, installation, and operating records supportr.

the conclusion that, with the exception of nozzle G on Accumulator 2-1, the Unit 2 sample and fill line nozzles ' leaked as a result of small base material intergranular stress corrosion cracks.

Cracking most likely was initiated because (1) sulfur and chloride contamination was present in the socket region _of the nozzles, (2) the 1091S/85K

i l

LICENSEE EVENT REPORT (LER) TEXT CONTINUATION 2026'72

\\

,Act u VV NAME (3)

DOCKET MJMBER (2)

(f8 NUMBER I8)

PAGE (3) l

",t'L"'

L"ll" DIABLO CANYON UNIT 2 0l5l0l0l0l3l2l3 87

- 0l2l3 0 l1 6 l 'l 10 1111 (a nozzles were highly sensitized, (3) the necessary aqueous environment was present, and (4) residual tensile stresses were present.

The basis for this conclusion is:

1.

DCPP accumulators were supplied with the fill and sample lines between the vessel and skirt coupling installed by the vendor.

Contaminants, most likely introduced as a result of fabrication (cutting oils, forming compounds, l

etc.) or contaminated hydrostatic testing water, were not I

removed during subsequent flushing because of the tight crevice between the pipe and the nozzle socket.

Moreover, the tight controls on water chenistry at DCPP for hydrostatic testing, startup flushing, and accumulator inventory praclude the introduction of contaminants subsequent to manufacture.

l 2.

The austenitic stainless steel nozzles were type 304 (i.e., not a low carbon grade) and were welded into the

- vessel prior to vessel post weld stress relief heat treatment.

Consequently, the nozzles underwent a heat treatment during stress relieving that would cause significant sensitization (carbide precipitation at the grain boundarias).

3.

Sensitized type 304 stainless steel in stagnant 2000 ppm borated water systems at room temperature has been shown to be highly susceptible to IGSCC in the presence of trace amounts of chlorides and sulfur oxyanions.

The primary contaminant identified was sulfur, along with some chlorides.

4.

High local residual tensile stresses were present.

These stresses were yield-stress-magnitude and were sufficient to initiate 1GSCC given the conditions of contaminates and sensitized structure. The stresses resulted from differential contraction between the stainless steel nozzle and the carbon steel vessel during cooling (nozzle to vessel welds; vessel was stress-relieved with nozzles in place) and from solidification and shrinkage stresses from welding (socket welds).

5.

The orientation of the identifiable indications responsible for leakage were longitudinal for all leaks except for nozzle G on Accumulator 2-1.

In that case, the leak is believed to have been caused by a weld defect (lack of fusion); in addition, the orientation was circumferential. Unlike the leaks for the D nozzles on Accumulators 2-2 and 2-4, there was no recurrence of 1091S/85K

LICENSEE EVENT REPORT (LER) TEXT CONTINUATION 2()2672 i

FAC3L3tv NAME (1)

DoCKEI NUMSER (2)

L(R NUMOfR 6)

D Ar.f (3)

"K"

~

DIABLO CANYON UNIT 2 0l5l0l0l0l3l2l3 87

- 0l2l3 0l1 7 l 'l 10 TEXT (17) leakage after weld repair.

i 6.

With the exception of the nozzle G leak identified above, leaks that were initially stopped after being repaired with weld metal leaked again seven months following repair.

IV.

Analysis of Event The sample and fill lines are anchored to the accumulator nozzles and skirt, forming a stiff piping segment.

Seismic loads would be expected to be low due to this stiff configuration, the anticipated response spectra, and no relative seismic displacement between the skirt and vessel nozzle.

Thermal stresses are negligible because the service temperature of the accumulator inventory is essentially at containment ambient temperature.

The applied-stress at the IGSCC location will, therefore, be primarily the result of pressure stress and should not exceed approximately 1500 psi tension and 870 psi shear. Accordingly, self-limiting _ residual stresses, rather than applied loads, contribute to crack initiation.

Defect propagation beyond the shoulder region of the socket was not likely to occur as substantiated by the characteristics of the leaks observed and the very low service stresses.

Joint loads due to accumulator internal pressure are significantly less than the expected shear capacity of the socket and neither defect propagation nor catastrophic failure (separation of pipe and nozzle) would be expected as i

the result of applied loads.

The consequences of the defect going undetected would be limited to a continued very small leak.

Early detection of a drop in accumulator level and/or pressure is provided by two channels for level detection and alarms.

It is concluded that the leaks and-nsociated defects would not preclude delivery of sufficient accumulator inventory to the reactor coolant system.

The accumulators would continue to perform their intended safety function.

Therefore, there were no adverse safety consequences or implications

}

resulting from this condition.

V.

Corrective Actions The leaking nozzle D on Accumulators 2-2 and 2-4 have been redesigned and replaced. The new design utilizes a butt welded connection and type 304L base material. The defective weld (lack of fusion) on nozzle G of Accumulator 2-1 has been weld repaired with no subsequent leakage.

The leaking nozzle G on Accumulator 2-3 was repaired by replacement of defective-nozzle material.

Attachments 1 and 2 summarize repairs performed un Units 1 and 2 accumulator nozzles during the IRS-and 2R4 refueling outages, respectively.

1091S/85K

LICENSEE EVENT REPORT (LER) TEXT CONTINUATION 202672.

l,

=cu r u,.t. m u.-t.,

nu o>

4cian m

=. ~

=

j DIABLO CANYON UNIT 2 0l5l0l0l0l3l2l3 87

- 0l2l3 0l1 8 l"l 10 itat (p) i An enhanced periodic inspection program for accumulator nozzles is being developed and will be performed during future refueling outages.

VI.

Additional Information A.

Accumulator tank data:

Delta Southern Manufacturer Westinghouse Vendor Carbon steel, with 304 stainless steel liner -

Material 1350 cubic feet Size B.

Previous LERs on similar events:

None.

C.

Attachments:

1.

Accumulator Nozzle Repair - Unit 1-2.

Accumulator Nozzle Repair - Unit 2

.ev, l

1091S/85K

LICENSEE EVENT REPORT (LER) TEXT CONTINUATION 202672

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un" wuSu DIABLO CANYON UNIT 2 0l5l0l0l0l3l2l3 87 Ol2l3 0l1 9 l 'l 10 TEXT (37)

ATTACHMENT 1 ACCUMULATOR NOZZLE REPAIR - UNIT 1 ACCUMU-NOZZLE CARBON REPAIR TEST LATOR CONTENT HISTORY HISTORY I

1-1 A

.05 NONE NRI 1-1 B

.05 NONE NRI 1-1 C-A

.028 NONE NRI 1-1 C-B

.028 NONE NRI 1-1 C-1A

.028 NONE NRI 1-1 C-13

.028 NONE NRI 1-1 D

004 NONE NRI 1-1 E

NONE NRI 1-1 G

.05 NONE NRI 1-2 A

.05 NONE NRI 1-2 B

.05 NONE NRI l

1-2 C-A

.027 NONE NRI 1-2 C-B

.027 NONE NRI 1-2 C-1A

.027 NONE NRI 1-2 C-1B

.027 NONE NRI 1-2 D

004 NONE NRI 4

1-2 E

BUFFED 1-IND 1-2 G

.05 NONE NRI 1-3 A

.05 NONE NRI 1-3 B

.03 NONE NRI 1-3 C-A

.047 NONE NRI 1-3 C-B

.047 NONE NRI 1-3 C-1A

.047 NONE NRI 1-3 C-1B

.047 NONE NRI 1-3 D

.004 NONE NRI 1-3 E

.024 NONE NRI 1-3 G

.03 NONE NRI 1-4 A

.05 NONE NRI 1-4 B

.03 NONE NRI l-4 C-A

.0473 NONE NRI 3

1-4 C-B

.047 REPLACED 2-IND 1-4 C-1A

.0473 NONE NRI 3

1-4 C-1B

.047 REPLACED 3-IND 1-4 D

.004 NONE NRI 1-4 E

.024 NONE NRI 1-4 G

.03 REPAIRED ROUNDED IND 1-4 G (skirt cpl)

REPLACED 1-IND l

l l

I No recordable indications l

2 Recorded data believed to be for F nozzle instead of E nozzle and, therefore, data may be in error.

l 3

Questionable or illegible 1091S/85K

202672 LICENSEE EVENT REPORT (LER) TEXT CONTINUATION c

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DOCECT NUMBER (2)

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PAGE (3) 1 naR maamm Reveun.

NUMER ORJMMR DIABLO CANYON UNIT 2 0l5l0l0l0l3l2l3 87 Ol2l3 0 l1 10 l 'l 10 TEXT (17)

ATTACHMENT 2 ACCUMULATOR NOZZLE REPAIR - UNIT 2 ACCUMU-NOZZLE CARBON REPAIR TEST LATOR CONTENT HISTORY HISTORY I

2 2-1 A

NONE NRI I

2-1 B

NONE NRI 1-IND 2-1 C-A

.05 gEPLACED 2-1 C-B

.05 NRI 2-1 C-1A

.05 NONE NRI 2-1 C-1B

.05 NONE NRI4 2-1 D

.05 NONE NRI 2-1 E

061 NONE NDI I

4 2-1 G

REPAIRED NRI 2-2 A

.04 NONE NRI 2-2 B

.04 REPAIRED 1-IND 2-2 C-A

.05 NONE NRI 2-2 C-B

.05 REPLACED 3-IND 2-2 C-1A

.05 NONE NRI 2-2 C-1B

.05 NONE NRI4 2-2 D

.05 REPLACED NRI 2-2 E

.061 NONE NRI4 2-2 G

.053 NONE NRI 2-3 A

.04 REPAIRED 1-IND 2-3 B

.04 NONE NRI 2-3 C-A

.05 NONE NRI 2-3 C-B

.05 NONE NRI 2-3 C-1A

.05 REPAIRED NRI 2-3 C-1B

.05 REPAIRED NRI 2-3 D

.05 REPLACED 2-IND

.m2-3 E

.061 NONE NRI;"

2-3 G

.04 NONE NRI 2-3 G (skirt cpl)

REPLACED 1-IND l

2-4 A

.04 REPAIRED 1-IND 2-4 B

.04 NONE NRI' 2-4 C-A

.05 NONE NRI 2-4 C-B

.05 NONE NRI 2-4 C-1A

.05 NONE NRI 2-4 C-1B

.05 NONE NRI I 2-4 D

. 0 5-REPLACED NRI 2-4 E

.061 NONE NRI 4 2-4 G

.04 NONE

, NRI i

l l

l I

Questionable or illegible l

2 No recordable indications 3

l Linear indication in 1985.

Accepted-as-is.

4 0

Limited examination due to bottom curvature.

Generally, only 180 scanned.

1091S/85K