Information Notice 2002-03, Highly Radioactive Particle Control Problems During Spent Fuel Pool Cleanout: Difference between revisions

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{{#Wiki_filter:UNITED STATES
{{#Wiki_filter:UNITED STATES


NUCLEAR REGULATORY COMMISSION
===NUCLEAR REGULATORY COMMISSION===
OFFICE OF NUCLEAR REACTOR REGULATION


OFFICE OF NUCLEAR REACTOR REGULATION
WASHINGTON, D.C.  20555-0001


WASHINGTON, D.C. 20555-0001 January 10, 2002 NRC INFORMATION NOTICE 2002-03:                 HIGHLY RADIOACTIVE PARTICLE CONTROL
===January 10, 2002===
NRC INFORMATION NOTICE 2002-03:


PROBLEMS DURING SPENT FUEL POOL
===HIGHLY RADIOACTIVE PARTICLE CONTROL===
PROBLEMS DURING SPENT FUEL POOL


CLEANOUT
CLEANOUT
Line 39: Line 42:
during removal of material from a spent fuel pool prior to shipping the material offsite for
during removal of material from a spent fuel pool prior to shipping the material offsite for


disposal. The issue emphasized in this notice is that highly radioactive (hot) particles represent
disposal. The issue emphasized in this notice is that highly radioactive (hot) particles represent


a radiological hazard not just in terms of shallow dose to the skin or an extremity but also as a
a radiological hazard not just in terms of shallow dose to the skin or an extremity but also as a


deep or whole-body dose. It is expected that recipients will review the information for
deep or whole-body dose. It is expected that recipients will review the information for


applicability to their facilities and consider actions, as appropriate, to avoid similar problems.
applicability to their facilities and consider actions, as appropriate, to avoid similar problems.
Line 54: Line 57:
Station completed compacting irradiated components that had been temporarily stored in the
Station completed compacting irradiated components that had been temporarily stored in the


pool. Working under water remotely, the licensee had used an advanced crusher and shearer
pool. Working under water remotely, the licensee had used an advanced crusher and shearer


(ACS) unit to compact control rod blades and local power range monitors. On October 12,
(ACS) unit to compact control rod blades and local power range monitors. On October 12,
2000, the ACS was removed from the cask storage pit with a crane after apparently inadequate
2000, the ACS was removed from the cask storage pit with a crane after apparently inadequate


cleaning with a high-pressure spray Hydrolazer. The ACS was moved over the refueling floor
cleaning with a high-pressure spray Hydrolazer. The ACS was moved over the refueling floor


and into the reactor head washdown area for further decontamination prior to shipment offsite.
and into the reactor head washdown area for further decontamination prior to shipment offsite.


The ACS was not totally wrapped or sealed during this movement. Also, access to the ACS
The ACS was not totally wrapped or sealed during this movement. Also, access to the ACS


pathway over the refueling floor was not radiologically controlled during the move.
pathway over the refueling floor was not radiologically controlled during the move.
Line 69: Line 72:
During the movement of the ACS, the refueling floor local area radiation monitor began to
During the movement of the ACS, the refueling floor local area radiation monitor began to


alarm. The cause was a previously unidentified highly radioactive particle which had fallen from
alarm. The cause was a previously unidentified highly radioactive particle which had fallen from


the ACS. The particle was later determined to be a 2.78 gigabecquerel (Gbq) [75 millicuries
the ACS. The particle was later determined to be a 2.78 gigabecquerel (Gbq) [75 millicuries


(mCi)] Co-60 particle, reading approximately 8 sievert/h (Sv/h) (800 rem/h) at contact.
(mCi)] Co-60 particle, reading approximately 8 sievert/h (Sv/h) (800 rem/h) at contact.
Line 77: Line 80:
The licensee stopped work, shielded and captured the particle, and initiated radioactive particle
The licensee stopped work, shielded and captured the particle, and initiated radioactive particle


control zone coverage for the entire refueling floor. Additional actions undertaken at that time
control zone coverage for the entire refueling floor. Additional actions undertaken at that time


included formation of a root cause event review team. The teams work led to upgraded
included formation of a root cause event review team. The teams work led to upgraded


controls, surveying, more management oversight and more detailed planning and work
controls, surveying, more management oversight and more detailed planning and work
Line 85: Line 88:
procedures for handling high specific activity particles.
procedures for handling high specific activity particles.


A search was then begun for additional hot particles on the refueling floor. Workers in particle
A search was then begun for additional hot particles on the refueling floor. Workers in particle


control zones were surveyed for particles every 15 minutes, and more protective clothing (PC)
control zones were surveyed for particles every 15 minutes, and more protective clothing (PC)
was required for certain work activities. The 15-minute control was a default stay time, and not
was required for certain work activities. The 15-minute control was a default stay time, and not


based on dose calculations for the high-activity particles known to be present.
based on dose calculations for the high-activity particles known to be present.
Line 94: Line 97:
During the cleanup activities, more than 30 radioactive particles were found on the refueling
During the cleanup activities, more than 30 radioactive particles were found on the refueling


floor. Two high activity radioactive particles found on September 9 and December 6, 2000, had
floor. Two high activity radioactive particles found on September 9 and December 6, 2000, had


resulted in shallow-dose equivalent (SDE) exposures of 0.12 and 0.17 Sv (12 and 17 rem),
resulted in shallow-dose equivalent (SDE) exposures of 0.12 and 0.17 Sv (12 and 17 rem),
which is below the annual SDE limit of 50 rem. The licensee discovered two more high-activity
which is below the annual SDE limit of 50 rem. The licensee discovered two more high-activity


particles, a 0.78 Gbq (21 mCi) particle on November 28, and a 0.7 Gbq (19 mCi) particle on
particles, a 0.78 Gbq (21 mCi) particle on November 28, and a 0.7 Gbq (19 mCi) particle on


December 4, 2000; these particles did not result in significant exposure to personnel. No actual
December 4, 2000; these particles did not result in significant exposure to personnel. No actual


exposures in excess of any annual dose limits occurred during the cleanup activities.
exposures in excess of any annual dose limits occurred during the cleanup activities.
Line 109: Line 112:
December 11-15, 2000 (Inspection Report Nos. 05000387/2000-009 and 05000388/2000-009, ADAMS Accession No. ML010250469), the NRC inspector identified significant weaknesses in
December 11-15, 2000 (Inspection Report Nos. 05000387/2000-009 and 05000388/2000-009, ADAMS Accession No. ML010250469), the NRC inspector identified significant weaknesses in


the licensees particle control program. The inspector noted that the licensee had failed to
the licensees particle control program. The inspector noted that the licensee had failed to


identify that conventional hand-held survey instruments using standard survey methods were
identify that conventional hand-held survey instruments using standard survey methods were
Line 119: Line 122:
The licensees evaluation had failed to consider properly and account for the potential for
The licensees evaluation had failed to consider properly and account for the potential for


substantial dose to personnel from the high-activity particles. Specifically, the 15-minute worker
substantial dose to personnel from the high-activity particles. Specifically, the 15-minute worker


stay time was not adequate to prevent potential overexposures from the particles known to be
stay time was not adequate to prevent potential overexposures from the particles known to be


present in and around the refueling floor. The stay time would have allowed both SDE and total
present in and around the refueling floor. The stay time would have allowed both SDE and total


effective dose equivalent (TEDE) annual exposure limits to be exceeded.
effective dose equivalent (TEDE) annual exposure limits to be exceeded.


Four of the particles found ranged from 0.7 to 2.78 Gbq (19 to 75 mCi). Had the particles been
Four of the particles found ranged from 0.7 to 2.78 Gbq (19 to 75 mCi). Had the particles been


directly on the workers PCs, the TEDE annual limit of 0.05 Sv (5 rem) could have been
directly on the workers PCs, the TEDE annual limit of 0.05 Sv (5 rem) could have been
Line 141: Line 144:
implemented improved training and communication of lessons learned in this area. Discussion
implemented improved training and communication of lessons learned in this area. Discussion


During previous similar processing of irradiated components at Susquehanna in 1991, radioactive particles had been identified with external gamma dose rates greater than
During previous similar processing of irradiated components at Susquehanna in 1991, radioactive particles had been identified with external gamma dose rates greater than


100 rem/hr. However, the plant failed to incorporate fully this previous experience and industry- wide experience into the planning for the 2000 fuel pool clean out project. (NRC Information
100 rem/hr. However, the plant failed to incorporate fully this previous experience and industry- wide experience into the planning for the 2000 fuel pool clean out project. (NRC Information


Notice No. 90-33, Sources of Unexpected Occupational Radiation Exposures at Spent Fuel
Notice No. 90-33, Sources of Unexpected Occupational Radiation Exposures at Spent Fuel
Line 152: Line 155:
had implemented were not sufficient under the circumstances to evaluate and control the
had implemented were not sufficient under the circumstances to evaluate and control the


potential radiological challenges posed by these extremely high activity particles. A Notice of
potential radiological challenges posed by these extremely high activity particles. A Notice of


Violation (failure to conduct adequate evaluation and survey) associated with a White finding
Violation (failure to conduct adequate evaluation and survey) associated with a White finding


(using the Significance Determination Process) was issued. These actions were taken because
(using the Significance Determination Process) was issued. These actions were taken because


of the substantial potential for exposure in excess of the annual limit for TEDE even though no
of the substantial potential for exposure in excess of the annual limit for TEDE even though no
Line 164: Line 167:
During the regulatory conference for this violation, the licensee stated that it needed to improve
During the regulatory conference for this violation, the licensee stated that it needed to improve


its hot particle surveying, identification, handling, and control. The improvements included
its hot particle surveying, identification, handling, and control. The improvements included


more effective use of remote handling techniques, proactive staging of particle control zones, and aggressive treatment of potential sources of particles by using decontamination and
more effective use of remote handling techniques, proactive staging of particle control zones, and aggressive treatment of potential sources of particles by using decontamination and
Line 172: Line 175:
The licensee noted that in cases like this where a contractor was used for a challenging
The licensee noted that in cases like this where a contractor was used for a challenging


radiological evolution, plant management oversight was essential. That oversight must focus
radiological evolution, plant management oversight was essential. That oversight must focus


on, and have sufficient resources to implement and maintain a sense of an acceptable radiation
on, and have sufficient resources to implement and maintain a sense of an acceptable radiation


culture and acceptable practices and standards for radiation work. According to the licensee, this can best be accomplished by direct ownership for significant, high-risk projects
culture and acceptable practices and standards for radiation work. According to the licensee, this can best be accomplished by direct ownership for significant, high-risk projects


demonstrated by the visible presence and direct oversight of the work by utility managers.
demonstrated by the visible presence and direct oversight of the work by utility managers.
Line 184: Line 187:
focus attention on the large potential doses from these challenging radiological work
focus attention on the large potential doses from these challenging radiological work


environments. The worker training program and job oversight must emphasize the most
environments. The worker training program and job oversight must emphasize the most


important lesson learned from the eventthat radioactive particles can present not only
important lesson learned from the eventthat radioactive particles can present not only
Line 190: Line 193:
shallow-dose risks but, at higher activity levels, whole body dose risks, which can be much
shallow-dose risks but, at higher activity levels, whole body dose risks, which can be much


more significant. This information notice requires no specific action or written response. If you have any
more significant. This information notice requires no specific action or written response. If you have any


questions about the information in this notice, please contact one of the technical contacts
questions about the information in this notice, please contact one of the technical contacts
Line 197: Line 200:


/RA/
/RA/
                                              William D. Beckner, Program Director


===William D. Beckner, Program Director===
Operating Reactor Improvements Program
Operating Reactor Improvements Program


Division of Regulatory Improvement Programs
===Division of Regulatory Improvement Programs===
Office of Nuclear Reactor Regulation


Office of Nuclear Reactor Regulation
Technical contacts:  James E. Wigginton, NRR


Technical contacts: James E. Wigginton, NRR                  James D. Noggle, Region I
===James D. Noggle, Region I===
301-415-1059
610-337-5063 E-mail: jew2@nrc.gov


301-415-1059                            610-337-5063 E-mail: jew2@nrc.gov                    E-mail: jdn@nrc.gov
E-mail: jdn@nrc.gov


Attachment: List of Recently Issued NRC Information Notices
Attachment: List of Recently Issued NRC Information Notices


ML011790547
ML011790547
*See previous concurrence
*See previous concurrence


OFFICE REXB               Tech Ed             IOLB           SC:REXB         RORP
OFFICE REXB
 
Tech Ed
 
IOLB
 
SC:REXB
 
RORP
 
NAME


NAME EGoodwin*           PKleene*           GTracy*       JTappert*       Wbeckner*
EGoodwin*
  DATE     12/20/2001      6/19/2001          8/20/2001      6/26/2001      01/08/2002
PKleene*
GTracy*
JTappert*
Wbeckner*
DATE


Attachment 1 LIST OF RECENTLY ISSUED
12/20/2001
6/19/2001
8/20/2001
6/26/2001
01/08/2002


______________________________________________________________________________________
OL = Operating License
CP = Construction Permit
===Attachment 1 LIST OF RECENTLY ISSUED===
NRC INFORMATION NOTICES
NRC INFORMATION NOTICES


_____________________________________________________________________________________
_____________________________________________________________________________________
Information                                         Date of
Information


Notice No.               Subject                   Issuance   Issued to
Date of
 
Notice No.
 
Subject
 
Issuance
 
Issued to


_____________________________________________________________________________________
_____________________________________________________________________________________
2002-02           Recent Experience with           01/08/2002  All holders of operating licenses
2002-02
 
===Recent Experience with===
Plugged Steam Generator
 
Tubes


Plugged Steam Generator                      for pressurized-water reactors
01/08/2002


Tubes                                        (PWRs), except those who have
===All holders of operating licenses===
for pressurized-water reactors
 
(PWRs), except those who have


permanently ceased operations
permanently ceased operations
Line 243: Line 289:
the reactor.
the reactor.


2002-01           Metalclad Switchgear Failures    01/08/2002  All holders of licenses for nuclear
2002-01


and Consequent Losses of                     power reactors.
===Metalclad Switchgear Failures===
and Consequent Losses of


Offsite Power
===Offsite Power===
01/08/2002


2001-19          Improper Maintenance and          12/17/2001  All holders of operating licenses
===All holders of licenses for nuclear===
power reactors.


Reassembly of Automatic Oil                   for nuclear power reactors, Bubblers                                      except those who have
2001-19
 
===Improper Maintenance and===
Reassembly of Automatic Oil
 
Bubblers
 
12/17/2001
 
===All holders of operating licenses===
for nuclear power reactors, except those who have


permanently ceased operations
permanently ceased operations
Line 261: Line 320:
the reactor vessel.
the reactor vessel.


2001-18           Degraded or Failed Automated     12/14/2001 All uranium fuel conversion, Electronic Monitoring, Control,              enrichment, and fabrication
2001-18
 
===Degraded or Failed Automated===
Electronic Monitoring, Control,
 
===Alarming, Response, and===
Communications Needed for
 
Safety and/or Safeguards
 
12/14/2001 All uranium fuel conversion, enrichment, and fabrication


Alarming, Response, and                      licensees and certificate holders
licensees and certificate holders


Communications Needed for                    authorized to receive safeguards
authorized to receive safeguards


Safety and/or Safeguards                      information. Information notice is
information. Information notice is


not available to the public
not available to the public
Line 275: Line 344:
information.
information.


2001-17           Degraded and Failed              12/14/2001  All uranium fuel conversion, Performance of Essential                      enrichment, and fabrication
2001-17


Utilities Needed for Safety and               licensees and certificate holders
===Degraded and Failed===
Performance of Essential


Safeguards                                   authorized to receive safeguards
===Utilities Needed for Safety and===
Safeguards


information. Information notice is
12/14/2001 All uranium fuel conversion, enrichment, and fabrication
 
licensees and certificate holders
 
authorized to receive safeguards
 
information. Information notice is


not available to the public
not available to the public
Line 289: Line 366:
information.
information.


2001-08,         Update on Radiation Therapy      11/20/2001  All medical licensees.
2001-08, Sup. 2


===Sup. 2            Overexposures in Panama===
===Update on Radiation Therapy===
2001-16          Recent Foreign and Domestic      steam      Tubes and Internals
Overexposures in Panama


Experience with Degradation of    Generator
11/20/2001 All medical licensees.


______________________________________________________________________________________
2001-16
OL = Operating License
 
===Recent Foreign and Domestic===
Experience with Degradation of
 
steam
 
Generator


CP = Construction Permit}}
Tubes and Internals}}


{{Information notice-Nav}}
{{Information notice-Nav}}

Latest revision as of 01:53, 17 January 2025

Highly Radioactive Particle Control Problems During Spent Fuel Pool Cleanout
ML011790547
Person / Time
Issue date: 01/10/2002
From: Beckner W
Operational Experience and Non-Power Reactors Branch
To:
References
TAC MB1382 IN-02-003
Download: ML011790547 (7)


UNITED STATES

NUCLEAR REGULATORY COMMISSION

OFFICE OF NUCLEAR REACTOR REGULATION

WASHINGTON, D.C. 20555-0001

January 10, 2002

NRC INFORMATION NOTICE 2002-03:

HIGHLY RADIOACTIVE PARTICLE CONTROL

PROBLEMS DURING SPENT FUEL POOL

CLEANOUT

Addressees

All holders of operating licenses for nuclear power reactors, holders of licenses for permanently

shutdown facilities with fuel onsite, and holders of licenses for non-power reactors.

Purpose

The U.S. Nuclear Regulatory Commission (NRC) is issuing this information notice to alert

addressees to recent issues involving evaluation and control of radioactive particles generated

during removal of material from a spent fuel pool prior to shipping the material offsite for

disposal. The issue emphasized in this notice is that highly radioactive (hot) particles represent

a radiological hazard not just in terms of shallow dose to the skin or an extremity but also as a

deep or whole-body dose. It is expected that recipients will review the information for

applicability to their facilities and consider actions, as appropriate, to avoid similar problems.

However, suggestions contained in this information notice are not NRC requirements; therefore, no specific action or written response is required.

Description of Circumstances

Toward the end of a 5-month spent fuel pool cleaning project, the Susquehanna Steam Electric

Station completed compacting irradiated components that had been temporarily stored in the

pool. Working under water remotely, the licensee had used an advanced crusher and shearer

(ACS) unit to compact control rod blades and local power range monitors. On October 12,

2000, the ACS was removed from the cask storage pit with a crane after apparently inadequate

cleaning with a high-pressure spray Hydrolazer. The ACS was moved over the refueling floor

and into the reactor head washdown area for further decontamination prior to shipment offsite.

The ACS was not totally wrapped or sealed during this movement. Also, access to the ACS

pathway over the refueling floor was not radiologically controlled during the move.

During the movement of the ACS, the refueling floor local area radiation monitor began to

alarm. The cause was a previously unidentified highly radioactive particle which had fallen from

the ACS. The particle was later determined to be a 2.78 gigabecquerel (Gbq) [75 millicuries

(mCi)] Co-60 particle, reading approximately 8 sievert/h (Sv/h) (800 rem/h) at contact.

The licensee stopped work, shielded and captured the particle, and initiated radioactive particle

control zone coverage for the entire refueling floor. Additional actions undertaken at that time

included formation of a root cause event review team. The teams work led to upgraded

controls, surveying, more management oversight and more detailed planning and work

procedures for handling high specific activity particles.

A search was then begun for additional hot particles on the refueling floor. Workers in particle

control zones were surveyed for particles every 15 minutes, and more protective clothing (PC)

was required for certain work activities. The 15-minute control was a default stay time, and not

based on dose calculations for the high-activity particles known to be present.

During the cleanup activities, more than 30 radioactive particles were found on the refueling

floor. Two high activity radioactive particles found on September 9 and December 6, 2000, had

resulted in shallow-dose equivalent (SDE) exposures of 0.12 and 0.17 Sv (12 and 17 rem),

which is below the annual SDE limit of 50 rem. The licensee discovered two more high-activity

particles, a 0.78 Gbq (21 mCi) particle on November 28, and a 0.7 Gbq (19 mCi) particle on

December 4, 2000; these particles did not result in significant exposure to personnel. No actual

exposures in excess of any annual dose limits occurred during the cleanup activities.

During a scheduled NRC health physics, rad-waste transportation, baseline inspection during

December 11-15, 2000 (Inspection Report Nos. 05000387/2000-009 and 05000388/2000-009, ADAMS Accession No. ML010250469), the NRC inspector identified significant weaknesses in

the licensees particle control program. The inspector noted that the licensee had failed to

identify that conventional hand-held survey instruments using standard survey methods were

underestimating the contact dose rates of the particles, thus underestimating the radiological

hazards not just to the skin but in terms of whole body exposure.

The licensees evaluation had failed to consider properly and account for the potential for

substantial dose to personnel from the high-activity particles. Specifically, the 15-minute worker

stay time was not adequate to prevent potential overexposures from the particles known to be

present in and around the refueling floor. The stay time would have allowed both SDE and total

effective dose equivalent (TEDE) annual exposure limits to be exceeded.

Four of the particles found ranged from 0.7 to 2.78 Gbq (19 to 75 mCi). Had the particles been

directly on the workers PCs, the TEDE annual limit of 0.05 Sv (5 rem) could have been

exceeded in 25 seconds to 2 minutes, and the SDE limit exceeded in 6 to 21 seconds, depending on the activity of the individual particle.

In response to the NRC findings and a 0.17 Sv (17 rem) SDE exposure on December 6 from a

particle on a workers boot, licensee management stopped all high-risk work, initiated a

comprehensive events evaluation, requested on-site assistance by an industry expert team, and

implemented improved training and communication of lessons learned in this area. Discussion

During previous similar processing of irradiated components at Susquehanna in 1991, radioactive particles had been identified with external gamma dose rates greater than

100 rem/hr. However, the plant failed to incorporate fully this previous experience and industry- wide experience into the planning for the 2000 fuel pool clean out project. (NRC Information

Notice No. 90-33, Sources of Unexpected Occupational Radiation Exposures at Spent Fuel

Storage Pools, also concerns highly radioactive particles.)

Prior to the NRC baseline inspection, after the initial event, the work controls that the licensee

had implemented were not sufficient under the circumstances to evaluate and control the

potential radiological challenges posed by these extremely high activity particles. A Notice of

Violation (failure to conduct adequate evaluation and survey) associated with a White finding

(using the Significance Determination Process) was issued. These actions were taken because

of the substantial potential for exposure in excess of the annual limit for TEDE even though no

worker dose limits were exceeded.

During the regulatory conference for this violation, the licensee stated that it needed to improve

its hot particle surveying, identification, handling, and control. The improvements included

more effective use of remote handling techniques, proactive staging of particle control zones, and aggressive treatment of potential sources of particles by using decontamination and

filtration on systems that communicate with the spent fuel pool.

The licensee noted that in cases like this where a contractor was used for a challenging

radiological evolution, plant management oversight was essential. That oversight must focus

on, and have sufficient resources to implement and maintain a sense of an acceptable radiation

culture and acceptable practices and standards for radiation work. According to the licensee, this can best be accomplished by direct ownership for significant, high-risk projects

demonstrated by the visible presence and direct oversight of the work by utility managers.

Most importantly, this occurrence demonstrated a need to strengthen procedural controls to

focus attention on the large potential doses from these challenging radiological work

environments. The worker training program and job oversight must emphasize the most

important lesson learned from the eventthat radioactive particles can present not only

shallow-dose risks but, at higher activity levels, whole body dose risks, which can be much

more significant. This information notice requires no specific action or written response. If you have any

questions about the information in this notice, please contact one of the technical contacts

listed below or the appropriate Office of Nuclear Reactor Regulation (NRR) project manager.

/RA/

William D. Beckner, Program Director

Operating Reactor Improvements Program

Division of Regulatory Improvement Programs

Office of Nuclear Reactor Regulation

Technical contacts: James E. Wigginton, NRR

James D. Noggle, Region I

301-415-1059

610-337-5063 E-mail: jew2@nrc.gov

E-mail: jdn@nrc.gov

Attachment: List of Recently Issued NRC Information Notices

ML011790547

  • See previous concurrence

OFFICE REXB

Tech Ed

IOLB

SC:REXB

RORP

NAME

EGoodwin*

PKleene*

GTracy*

JTappert*

Wbeckner*

DATE

12/20/2001

6/19/2001

8/20/2001

6/26/2001

01/08/2002

______________________________________________________________________________________

OL = Operating License

CP = Construction Permit

Attachment 1 LIST OF RECENTLY ISSUED

NRC INFORMATION NOTICES

_____________________________________________________________________________________

Information

Date of

Notice No.

Subject

Issuance

Issued to

_____________________________________________________________________________________

2002-02

Recent Experience with

Plugged Steam Generator

Tubes

01/08/2002

All holders of operating licenses

for pressurized-water reactors

(PWRs), except those who have

permanently ceased operations

and have certified that fuel has

been permanently removed from

the reactor.

2002-01

Metalclad Switchgear Failures

and Consequent Losses of

Offsite Power

01/08/2002

All holders of licenses for nuclear

power reactors.

2001-19

Improper Maintenance and

Reassembly of Automatic Oil

Bubblers

12/17/2001

All holders of operating licenses

for nuclear power reactors, except those who have

permanently ceased operations

and have certified that fuel has

been permanently removed from

the reactor vessel.

2001-18

Degraded or Failed Automated

Electronic Monitoring, Control,

Alarming, Response, and

Communications Needed for

Safety and/or Safeguards

12/14/2001 All uranium fuel conversion, enrichment, and fabrication

licensees and certificate holders

authorized to receive safeguards

information. Information notice is

not available to the public

because it contains safeguards

information.

2001-17

Degraded and Failed

Performance of Essential

Utilities Needed for Safety and

Safeguards

12/14/2001 All uranium fuel conversion, enrichment, and fabrication

licensees and certificate holders

authorized to receive safeguards

information. Information notice is

not available to the public

because it contains safeguards

information.

2001-08, Sup. 2

Update on Radiation Therapy

Overexposures in Panama

11/20/2001 All medical licensees.

2001-16

Recent Foreign and Domestic

Experience with Degradation of

steam

Generator

Tubes and Internals