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Detroit Edison Company
Detroit Edison Company
6400 North Dixie Highway
6400 North Dixie Highway
Newport, MI 48166
Newport, MI 48166
SUBJECT:         FERMI POWER PLANT, UNIT 2, NRC INTEGRATED
SUBJECT:
                INSPECTION REPORT 05000341/2006003
FERMI POWER PLANT, UNIT 2, NRC INTEGRATED  
INSPECTION REPORT 05000341/2006003
Dear Mr. Cobb:
Dear Mr. Cobb:
On June 30, 2006, the U.S. Nuclear Regulatory Commission (NRC) completed an integrated
On June 30, 2006, the U.S. Nuclear Regulatory Commission (NRC) completed an integrated
inspection at your Fermi Power Plant, Unit 2. The enclosed report documents the inspection
inspection at your Fermi Power Plant, Unit 2. The enclosed report documents the inspection
findings which were discussed on July 11, 2006, with you and other members of your staff.
findings which were discussed on July 11, 2006, with you and other members of your staff.
The inspection examined activities conducted under your license as they relate to safety and to
The inspection examined activities conducted under your license as they relate to safety and to
compliance with the Commissions rules and regulations and with the conditions of your license.
compliance with the Commissions rules and regulations and with the conditions of your license.  
The inspectors reviewed selected procedures and records, observed activities, and interviewed
The inspectors reviewed selected procedures and records, observed activities, and interviewed
personnel.
personnel.
Based on the results of this inspection, five findings of very low safety significance were
Based on the results of this inspection, five findings of very low safety significance were
identified, all of which involved violations of NRC requirements. However, because these
identified, all of which involved violations of NRC requirements. However, because these
findings were of very low safety significance and because the issues were entered into your
findings were of very low safety significance and because the issues were entered into your
corrective program, the NRC is treating these findings as Non-Cited Violations in accordance
corrective program, the NRC is treating these findings as Non-Cited Violations in accordance
with Section VI.A.1 of the NRCs Enforcement Policy. If you contest the subject or severity of
with Section VI.A.1 of the NRCs Enforcement Policy. If you contest the subject or severity of
a Non-Cited Violation, you should provide a response within 30 days of the date of this
a Non-Cited Violation, you should provide a response within 30 days of the date of this
inspection report, with the basis for your denial, to the U.S. Nuclear Regulatory Commission,
inspection report, with the basis for your denial, to the U.S. Nuclear Regulatory Commission,
ATTN: Document Control Desk, Washington, DC 20555-0001, with a copy to the Regional
ATTN: Document Control Desk, Washington, DC 20555-0001, with a copy to the Regional
Administrator, U.S. Nuclear Regulatory Commission - Region III, 2443 Warrenville Road,
Administrator, U.S. Nuclear Regulatory Commission - Region III, 2443 Warrenville Road,
Suite 210, Lisle, IL 60532-4352; the Director, Office of Enforcement, U.S. Nuclear Regulatory
Suite 210, Lisle, IL 60532-4352; the Director, Office of Enforcement, U.S. Nuclear Regulatory
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facility.
facility.
In accordance with 10 CFR 2.390 of the NRCs Rules of Practice, a copy of this letter and
In accordance with 10 CFR 2.390 of the NRCs Rules of Practice, a copy of this letter and
its enclosure will be made available electronically for public inspection in the NRC Public
its enclosure will be made available electronically for public inspection in the NRC Public  


D. Cobb                                         -2-
D. Cobb
-2-
Document Room or from the Publicly Available Records (PARS) component of NRCs
Document Room or from the Publicly Available Records (PARS) component of NRCs
document system (ADAMS). ADAMS is accessible from the NRC Web site at
document system (ADAMS). ADAMS is accessible from the NRC Web site at
http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room).
http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room).
                                            Sincerely,
Sincerely,
                                            /RA/
/RA/
                                            Christine A. Lipa, Chief
Christine A. Lipa, Chief
                                            Branch 4
Branch 4
                                            Division of Reactor Projects
Division of Reactor Projects
Docket No. 50-341
Docket No. 50-341
License No. NPF-43
License No. NPF-43
Enclosure:     Inspection Report 05000341/2006003
Enclosure:
                w/Attachment: Supplemental Information
Inspection Report 05000341/2006003
cc w/encl:     K. Hlavaty, Plant Manager
  w/Attachment: Supplemental Information
              R. Gaston, Manager, Nuclear Licensing
cc w/encl:
              D. Pettinari, Legal Department
K. Hlavaty, Plant Manager
              Michigan Department of Environmental Quality
R. Gaston, Manager, Nuclear Licensing
                Waste and Hazardous Materials Division
D. Pettinari, Legal Department
              M. Yudasz, Jr., Director, Monroe County
Michigan Department of Environmental Quality
                Emergency Management Division
  Waste and Hazardous Materials Division
              Supervisor - Electric Operators
M. Yudasz, Jr., Director, Monroe County
              State Liaison Officer, State of Michigan
  Emergency Management Division
              Wayne County Emergency Management Division
Supervisor - Electric Operators
State Liaison Officer, State of Michigan
Wayne County Emergency Management Division


D. Cobb                                                                       -2-
D. Cobb
-2-
Document Room or from the Publicly Available Records (PARS) component of NRCs
Document Room or from the Publicly Available Records (PARS) component of NRCs
document system (ADAMS). ADAMS is accessible from the NRC Web site at
document system (ADAMS). ADAMS is accessible from the NRC Web site at
http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room).
http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room).
                                                                          Sincerely,
Sincerely,
                                                                          Christine A. Lipa, Chief
Christine A. Lipa, Chief
                                                                          Branch 4
Branch 4
                                                                          Division of Reactor Projects
Division of Reactor Projects
Docket No. 50-341
Docket No. 50-341
License No. NPF-43
License No. NPF-43
Enclosure:               Inspection Report 05000341/2006003
Enclosure:
                            w/Attachment: Supplemental Information
Inspection Report 05000341/2006003
cc w/encl:               K. Hlavaty, Plant Manager
  w/Attachment: Supplemental Information
                          R. Gaston, Manager, Nuclear Licensing
cc w/encl:
                          D. Pettinari, Legal Department
K. Hlavaty, Plant Manager
                          Michigan Department of Environmental Quality
R. Gaston, Manager, Nuclear Licensing
                            Waste and Hazardous Materials Division
D. Pettinari, Legal Department
                          M. Yudasz, Jr., Director, Monroe County
Michigan Department of Environmental Quality
                            Emergency Management Division
  Waste and Hazardous Materials Division
                          Supervisor - Electric Operators
M. Yudasz, Jr., Director, Monroe County
                          State Liaison Officer, State of Michigan
  Emergency Management Division
                          Wayne County Emergency Management Division
Supervisor - Electric Operators
DOCUMENT NAME:E:\Filenet\ML062160540.wpd
State Liaison Officer, State of Michigan
G Publicly Available                       G Non-Publicly Available                   G Sensitive             G Non-Sensitive
Wayne County Emergency Management Division
To receive a copy of this document, indicate in the concurrence box "C" = Copy without attach/encl "E" = Copy with attach/encl "N" = No copy
DOCUMENT NAME:E:\\Filenet\\ML062160540.wpd
OFFICE             RIII                                 RIII
G Publicly Available
NAME               RLerch:dtp                           CLipa
G Non-Publicly Available
DATE               08/02/06                             08/02/06
G Sensitive
                                                          OFFICIAL RECORD COPY
G Non-Sensitive
To receive a copy of this document, indicate in the concurrence box "C" = Copy without attach/encl "E" = Copy with attach/encl "N" = No copy
OFFICE
RIII
RIII
NAME
RLerch:dtp
CLipa
DATE
08/02/06
08/02/06
OFFICIAL RECORD COPY


Donald K. Cobb                               -3-
Donald K. Cobb
-3-
ADAMS Distribution:
ADAMS Distribution:
LXR1
LXR1
Line 120: Line 137:
ROPreports@nrc.gov (inspection reports, final SDP letters, any letter with an IR number)
ROPreports@nrc.gov (inspection reports, final SDP letters, any letter with an IR number)


          U. S. NUCLEAR REGULATORY COMMISSION
Enclosure
                          REGION III
U. S. NUCLEAR REGULATORY COMMISSION
Docket No:           50-341
REGION III
License No:         NPF-43
Docket No:
Report No:           05000341/2006003
50-341
Licensee:           Detroit Edison Company
License No:
Facility:           Fermi Power Plant, Unit 2
NPF-43
Location:           Newport, Michigan
Report No:
Dates:               April 1 through June 30, 2006
05000341/2006003
Inspectors:         R. Michael Morris, Senior Resident Inspector
Licensee:
                    T. Steadham, Resident Inspector
Detroit Edison Company
                    A. Wilson, NRC Headquarters
Facility:
                    M. Franke, Senior Resident Inspector, Perry
Fermi Power Plant, Unit 2
                    M. Jordan, NRC Consultant
Location:
                    R. Langstaff, Senior Reactor Inspector
Newport, Michigan
                    M. Mitchell, Radiation Specialist
Dates:
Approved by:         C. Lipa, Chief
April 1 through June 30, 2006
                    Branch 4
Inspectors:
                    Division of Reactor Projects
R. Michael Morris, Senior Resident Inspector
                                                                  Enclosure
T. Steadham, Resident Inspector
A. Wilson, NRC Headquarters
M. Franke, Senior Resident Inspector, Perry
M. Jordan, NRC Consultant
R. Langstaff, Senior Reactor Inspector
M. Mitchell, Radiation Specialist
Approved by:
C. Lipa, Chief
Branch 4
Division of Reactor Projects


                                      SUMMARY OF FINDINGS
Enclosure
2
SUMMARY OF FINDINGS
IR 05000341/2006003; 04/01/2006-06/30/2006; Fermi Power Plant, Unit 2; Fire Protection,
IR 05000341/2006003; 04/01/2006-06/30/2006; Fermi Power Plant, Unit 2; Fire Protection,
Maintenance Risk Assessment, Operability Evaluations, Refueling and Outage Activities.
Maintenance Risk Assessment, Operability Evaluations, Refueling and Outage Activities.
This report covers a 3-month period of inspection by resident inspectors and announced
This report covers a 3-month period of inspection by resident inspectors and announced
baseline inspections by a regional radiation specialist inspector. Five Green findings, all of
baseline inspections by a regional radiation specialist inspector. Five Green findings, all of
which were associated with non-cited violations (NCVs) were identified. The significance of
which were associated with non-cited violations (NCVs) were identified. The significance of
most findings is indicated by their color (Green, White, Yellow, Red) using Inspection
most findings is indicated by their color (Green, White, Yellow, Red) using Inspection
Manual Chapter 0609, Significance Determination Process (SDP). Findings for which the
Manual Chapter 0609, Significance Determination Process (SDP). Findings for which the
SDP does not apply may be Green after NRC management review. The NRCs program for
SDP does not apply may be Green after NRC management review. The NRCs program for
overseeing the safe operation of commercial nuclear power reactors is described in
overseeing the safe operation of commercial nuclear power reactors is described in
NUREG-1649, Reactor Oversight Process, Revision 3, dated July 2000.
NUREG-1649, Reactor Oversight Process, Revision 3, dated July 2000.
A.     NRC-Identified and Self-Revealed Findings
A.
        Cornerstone: Initiating Events
NRC-Identified and Self-Revealed Findings
*       Green. The inspectors identified an NCV of 10 CFR 50.65(a)(4) for the failure to
Cornerstone: Initiating Events
        perform an adequate risk assessment for the Division I battery load test. The licensee
*
        failed to consider the effect the test would have on the temperature in the reactor
Green. The inspectors identified an NCV of 10 CFR 50.65(a)(4) for the failure to
        protection system motor generator set rooms. Consequently, the load bank used for the
perform an adequate risk assessment for the Division I battery load test. The licensee
        test caused the room temperature to increase which necessitated the unanticipated
failed to consider the effect the test would have on the temperature in the reactor
        installation of a temporary fan to cool the room. The licensee entered this issue into
protection system motor generator set rooms. Consequently, the load bank used for the
        their corrective action program to evaluate any programmatic or procedural deficiencies
test caused the room temperature to increase which necessitated the unanticipated
        that may have contributed to this event.
installation of a temporary fan to cool the room. The licensee entered this issue into
        This finding is more than minor because the licensees risk assessment failed to
their corrective action program to evaluate any programmatic or procedural deficiencies
        consider maintenance activities that could increase the likelihood of an initiating event,
that may have contributed to this event.
        specifically a loss of shutdown cooling from a reactor protection system motor generator
This finding is more than minor because the licensees risk assessment failed to
        set trip on high temperature. The finding is of very low safety significance because it did
consider maintenance activities that could increase the likelihood of an initiating event,
        not affect the ability of operators to recover from a loss of shutdown cooling if it had
specifically a loss of shutdown cooling from a reactor protection system motor generator
        occurred. The cause of the finding is related to the cross-cutting element of Human
set trip on high temperature. The finding is of very low safety significance because it did
        Performance. (Section 1R13.2)
not affect the ability of operators to recover from a loss of shutdown cooling if it had
        Cornerstone: Mitigating Systems
occurred. The cause of the finding is related to the cross-cutting element of Human
*       Green. The inspectors identified an NCV of license condition 2.C(9) due to the
Performance. (Section 1R13.2)
        presence of unauthorized transient combustible materials in the residual heat removal
Cornerstone: Mitigating Systems
        complex. An office chair and a plastic trash bin half filled with paper were secured next
*
        to the electrical panel and associated cable raceway for emergency diesel generator 12
Green. The inspectors identified an NCV of license condition 2.C(9) due to the
        ventilation in the emergency diesel generator 12 switchgear room. The licensee entered
presence of unauthorized transient combustible materials in the residual heat removal
        this issue into their corrective action program and removed the unauthorized transient
complex. An office chair and a plastic trash bin half filled with paper were secured next
        combustible materials from the residual heat removal complex.
to the electrical panel and associated cable raceway for emergency diesel generator 12
        This finding is more than minor because it affected the Mitigating Systems Cornerstone
ventilation in the emergency diesel generator 12 switchgear room. The licensee entered
        attribute for protection against external factors. Specifically, a fire involving the
this issue into their corrective action program and removed the unauthorized transient
        unauthorized transient combustibles could have affected a nearby electrical panel and
combustible materials from the residual heat removal complex.
        associated cable raceway containing mitigating system equipment important to safety.
This finding is more than minor because it affected the Mitigating Systems Cornerstone
                                                  2                                        Enclosure
attribute for protection against external factors. Specifically, a fire involving the
unauthorized transient combustibles could have affected a nearby electrical panel and
associated cable raceway containing mitigating system equipment important to safety.  


  The finding is of very low safety significance because the unauthorized transient
Enclosure
  combustible materials would not have ignited from existing sources of heat or electrical
3
  energy. The cause of the finding is related to the cross-cutting element of Problem
The finding is of very low safety significance because the unauthorized transient
  Identification and Resolution. (Section 1R05.2)
combustible materials would not have ignited from existing sources of heat or electrical
* Green. The inspectors identified an NCV of Technical Specification 3.1.5.a.2,
energy. The cause of the finding is related to the cross-cutting element of Problem
  Amendment 38, for the standby liquid control (SLC) system being inoperable for longer
Identification and Resolution. (Section 1R05.2)
  than the allowed time without the plant being placed in hot shutdown. The licensee
*
  failed to properly evaluate the operability of SLC during sparging activities when the
Green. The inspectors identified an NCV of Technical Specification 3.1.5.a.2,
  issue was raised in 1999. As a result, the licensee initiated a 21-hour sparge on the
Amendment 38, for the standby liquid control (SLC) system being inoperable for longer
  SLC tank on August 24, 1999, and failed to take actions in accordance with the
than the allowed time without the plant being placed in hot shutdown. The licensee
  Technical Specifications. After the deficient evaluation was identified on June 1, 2006,
failed to properly evaluate the operability of SLC during sparging activities when the
  the licensee revised the applicable procedures to declare the SLC system inoperable
issue was raised in 1999. As a result, the licensee initiated a 21-hour sparge on the
  during sparging the SLC tank. The licensee entered this issue into their corrective
SLC tank on August 24, 1999, and failed to take actions in accordance with the
  action program.
Technical Specifications. After the deficient evaluation was identified on June 1, 2006,
  This finding is more than minor because it represented a programmatic deficiency in the
the licensee revised the applicable procedures to declare the SLC system inoperable
  licensees chemical control program which affected the ability of the fire brigade to
during sparging the SLC tank. The licensee entered this issue into their corrective
  respond to and mitigate the effects of a fire. Upon management review, the finding is of
action program.
  very low safety significance because the quantities of the relevant chemicals were low
This finding is more than minor because it represented a programmatic deficiency in the
  and the storage location was sufficiently remote from mitigating equipment.
licensees chemical control program which affected the ability of the fire brigade to
  (Section 1R05.3)
respond to and mitigate the effects of a fire. Upon management review, the finding is of
  Cornerstone: Emergency Preparedness
very low safety significance because the quantities of the relevant chemicals were low
* Green. The inspectors identified an NCV of license condition 2.C(9), for the failure to
and the storage location was sufficiently remote from mitigating equipment.  
  appropriately store chemicals in accordance with the fire hazards analysis. The licensee
(Section 1R05.3)
  failed to evaluate the fire fighting response guidelines in NFPA-49 for various chemicals
Cornerstone: Emergency Preparedness
  brought into the protective area and, therefore, failed to appropriately store them as
*
  required by the licensees fire hazards analysis. As a result, five normally stored
Green. The inspectors identified an NCV of license condition 2.C(9), for the failure to
  chemicals in the building have recommended fire fighting strategies that are inconsistent
appropriately store chemicals in accordance with the fire hazards analysis. The licensee
  with the licensees approved fire protection pre-plan. The licensee entered this issue
failed to evaluate the fire fighting response guidelines in NFPA-49 for various chemicals
  into their correction action program.
brought into the protective area and, therefore, failed to appropriately store them as
  This finding is more than minor because it affected the equipment performance attribute
required by the licensees fire hazards analysis. As a result, five normally stored
  of the reactor safety cornerstone objective of ensuring the availability, reliability, and
chemicals in the building have recommended fire fighting strategies that are inconsistent
  capability of mitigating equipment to respond to initiating events to prevent undesirable
with the licensees approved fire protection pre-plan. The licensee entered this issue
  consequences. The finding is of very low safety significance because the total time of
into their correction action program.
  sparging activities was short. (Section 1R15.2)
This finding is more than minor because it affected the equipment performance attribute
  Cornerstone: Occupational Radiation Safety
of the reactor safety cornerstone objective of ensuring the availability, reliability, and
* Green. A self-revealed NCV was identified for the licensees failure to comply with
capability of mitigating equipment to respond to initiating events to prevent undesirable
  Technical Specification 5.4.1.a, written procedures shall be established, implemented,
consequences. The finding is of very low safety significance because the total time of
  and maintained covering applicable procedures recommended in Regulatory
sparging activities was short. (Section 1R15.2)
  Guide 1.33. The licensee did not adequately control the modification of the ventilation
Cornerstone: Occupational Radiation Safety
  equipment used to vent airborne radioactive particulate to the refuel floor during reactor
*
  vessel floodup. Consequently, while raising reactor vessel water level, the improper
Green. A self-revealed NCV was identified for the licensees failure to comply with
  venting led to personnel contaminations, uptakes of radioactive material, and the
Technical Specification 5.4.1.a, written procedures shall be established, implemented,
                                            3                                        Enclosure
and maintained covering applicable procedures recommended in Regulatory
Guide 1.33. The licensee did not adequately control the modification of the ventilation
equipment used to vent airborne radioactive particulate to the refuel floor during reactor
vessel floodup. Consequently, while raising reactor vessel water level, the improper
venting led to personnel contaminations, uptakes of radioactive material, and the


  evacuation of the Reactor Building. The licensee entered this issue into their corrective
Enclosure
  action program and conducted an investigation into the event. The corrective actions
4
  recommended the development and implementation of an acceptable methodology for
evacuation of the Reactor Building. The licensee entered this issue into their corrective
  raising reactor water level.
action program and conducted an investigation into the event. The corrective actions
  This finding is more than minor because it affected the Occupational Radiation Safety
recommended the development and implementation of an acceptable methodology for
  Cornerstone of Radiation Safety due to individual worker unplanned, unintended dose.
raising reactor water level.
  The finding was evaluated using the SDP and was determined to be a finding of very
This finding is more than minor because it affected the Occupational Radiation Safety
  low safety significance because there was not a substantial potential for overexposure
Cornerstone of Radiation Safety due to individual worker unplanned, unintended dose.  
  and the licensees ability to assess dose was not compromised. (Section 1R20)
The finding was evaluated using the SDP and was determined to be a finding of very
B. Licensee-Identified Violations
low safety significance because there was not a substantial potential for overexposure
  A violation of very low safety significance, which was identified by the licensee, has been
and the licensees ability to assess dose was not compromised. (Section 1R20)
  reviewed by the inspectors. Corrective actions taken or planned by the licensee have
B.
  been entered into the licensees corrective action program. This violation and corrective
Licensee-Identified Violations
  actions are listed in Section 4OA7 of this report.
A violation of very low safety significance, which was identified by the licensee, has been
                                            4                                      Enclosure
reviewed by the inspectors. Corrective actions taken or planned by the licensee have
been entered into the licensees corrective action program. This violation and corrective
actions are listed in Section 4OA7 of this report.


                                    REPORT DETAILS
Enclosure
    Summary of Plant Status
5
    Unit 2 began this inspection period shutdown for refueling outage 11 (RF11). Reactor
REPORT DETAILS
    startup began on May 3 but was halted at 95 percent power on May 9 due to indications
Summary of Plant Status
    of a fuel leak. Suppression testing commenced that same day, reducing reactor power
Unit 2 began this inspection period shutdown for refueling outage 11 (RF11). Reactor
    to approximately 63 percent until May 12 when the operators began increasing reactor
startup began on May 3 but was halted at 95 percent power on May 9 due to indications
    power after suppressing the fuel leak. On May 14, the reactor was at full power where it
of a fuel leak. Suppression testing commenced that same day, reducing reactor power
    remained at or near until May 19 when the operators began a reactor shutdown to
to approximately 63 percent until May 12 when the operators began increasing reactor
    replace the leaking fuel assembly. After completing the work, operators began a reactor
power after suppressing the fuel leak. On May 14, the reactor was at full power where it
    startup on May 28. The reactor reached full power on May 30 where it remained at or
remained at or near until May 19 when the operators began a reactor shutdown to
    near until June 15 when an automatic reactor scram occurred as a result of a failure of
replace the leaking fuel assembly. After completing the work, operators began a reactor
    main unit transformer 2B. The failed transformer was disconnected and reactor startup
startup on May 28. The reactor reached full power on May 30 where it remained at or
    began on June 16. On June 21, the reactor reached 63 percent power (maximum
near until June 15 when an automatic reactor scram occurred as a result of a failure of
    planned with transformer 2B out of service) and remained there for the remainder of the
main unit transformer 2B. The failed transformer was disconnected and reactor startup
    inspection period.
began on June 16. On June 21, the reactor reached 63 percent power (maximum
1.   REACTOR SAFETY
planned with transformer 2B out of service) and remained there for the remainder of the
    Cornerstone: Mitigating Systems, Barrier Integrity, Initiating Events, Emergency
inspection period.
    Preparedness
1.
1R01 Adverse Weather (71111.01A)
REACTOR SAFETY
a. Inspection Scope
Cornerstone: Mitigating Systems, Barrier Integrity, Initiating Events, Emergency
    The inspectors reviewed licensee procedures for mitigating the effects of hot weather.
Preparedness
    The inspectors reviewed severe weather procedures, emergency plan implementing
1R01
    procedures related to severe weather, and annunciator response procedures, and
Adverse Weather (71111.01A)
    performed walkdowns. This included the reactor building and turbine building ventilation
  a.  
    preparations. Additionally, the inspectors reviewed condition assessment resolution
Inspection Scope
    documents (CARD) and verified problems associated with adverse weather were
The inspectors reviewed licensee procedures for mitigating the effects of hot weather.
    entered into the corrective action program with the appropriate significance
The inspectors reviewed severe weather procedures, emergency plan implementing
    characterization.
procedures related to severe weather, and annunciator response procedures, and
    These activities represented one hot weather systems preparation inspection sample.
performed walkdowns. This included the reactor building and turbine building ventilation
b. Findings
preparations. Additionally, the inspectors reviewed condition assessment resolution
    No findings of significance were identified.
documents (CARD) and verified problems associated with adverse weather were
                                              5                                    Enclosure
entered into the corrective action program with the appropriate significance
characterization.
These activities represented one hot weather systems preparation inspection sample.
  b.  
Findings
 
No findings of significance were identified.


1R04 Equipment Alignments (71111.04)
Enclosure
.1   Partial System Walkdowns (71111.04Q)
6
   a. Inspection Scope
1R04
    The inspectors performed partial system walkdowns of the following risk-significant
Equipment Alignments (71111.04)
    systems:
.1
    C       Safety Relief Valves performed the week of April 3, 2006;
Partial System Walkdowns (71111.04Q)
    C       SLC A performed the week of April 24, 2006;
   a.
    C       Division II Residual Heal Removal (RHR) and Residual Heat Removal Service
Inspection Scope
            Water (RHRSW) Lineup performed the week of May 14, 2006;
The inspectors performed partial system walkdowns of the following risk-significant
    C       Standby Electrical Power (emergency diesel generator [EDG]) lineup performed
systems:
            the week of May 14, 2006; and
C
    C       Division I RHR and RHRSW Shutdown Cooling performed the week of
Safety Relief Valves performed the week of April 3, 2006;
            May 21, 2006.
C
    The inspectors selected these systems based on their risk significance relative to the
SLC A performed the week of April 24, 2006;
    reactor safety cornerstones. The inspectors reviewed operating procedures, system
C
    diagrams, Technical Specification (TS) requirements, Administrative TS, and the impact
Division II Residual Heal Removal (RHR) and Residual Heat Removal Service
    of ongoing work activities on redundant trains of equipment in order to identify
Water (RHRSW) Lineup performed the week of May 14, 2006;
    conditions that could have rendered the systems incapable of performing their intended
C
    functions. The inspectors also walked down accessible portions of the systems to verify
Standby Electrical Power (emergency diesel generator [EDG]) lineup performed
    system components were aligned correctly.
the week of May 14, 2006; and  
    In addition, the inspectors verified equipment alignment problems were entered into the
C
    corrective action program with the appropriate significance characterization.
Division I RHR and RHRSW Shutdown Cooling performed the week of
    These activities represented five quarterly partial system walkdown inspection samples.
May 21, 2006.  
   b. Findings
    No findings of significance were identified.
The inspectors selected these systems based on their risk significance relative to the
.2   Complete System Walkdown (71111.04S)
reactor safety cornerstones. The inspectors reviewed operating procedures, system
   a. Inspection Scope
diagrams, Technical Specification (TS) requirements, Administrative TS, and the impact
    The inspectors performed a complete system walkdown of the following risk-significant
of ongoing work activities on redundant trains of equipment in order to identify
    system:
conditions that could have rendered the systems incapable of performing their intended
    *       General Service Water (GSW) performed the week of April 24, 2006
functions. The inspectors also walked down accessible portions of the systems to verify
    The inspectors reviewed operating procedures, system diagrams, TS requirements, and
system components were aligned correctly.
    applicable sections of the Updated Final Safety Analysis Report (UFSAR) to ensure the
In addition, the inspectors verified equipment alignment problems were entered into the
    correct system lineup. The inspectors verified acceptable material condition of system
corrective action program with the appropriate significance characterization.
    components, availability of electrical power to system components, and that ancillary
These activities represented five quarterly partial system walkdown inspection samples.
    equipment or debris did not interfere with system performance.
   b.
                                              6                                    Enclosure
Findings
No findings of significance were identified.
.2
Complete System Walkdown (71111.04S)
   a.
Inspection Scope
The inspectors performed a complete system walkdown of the following risk-significant
system:
*
General Service Water (GSW) performed the week of April 24, 2006
The inspectors reviewed operating procedures, system diagrams, TS requirements, and
applicable sections of the Updated Final Safety Analysis Report (UFSAR) to ensure the
correct system lineup. The inspectors verified acceptable material condition of system
components, availability of electrical power to system components, and that ancillary
equipment or debris did not interfere with system performance.


    These activities represented one semi-annual complete system walkdown inspection
Enclosure
    sample.
7
   b. Findings
These activities represented one semi-annual complete system walkdown inspection
    No findings of significance were identified.
sample.
1R05 Fire Protection (71111.05)
   b.
.1   Routine Resident Inspector Tours (71111.05Q)
Findings
   a. Inspection Scope
No findings of significance were identified.
    The inspectors conducted fire protection tours of the following risk-significant plant
1R05
    areas:
Fire Protection (71111.05)
    *       Condensate Pump Room;
.1
    *       Standby Gas Treatment, Pipe Room;
Routine Resident Inspector Tours (71111.05Q)
    *       Top of Torus;
   a.  
    *       RHR Complex, Division I RHR;
Inspection Scope
    *       RHR Complex, Division I EDG, Switchgear Rooms, Ventilation Rooms;
The inspectors conducted fire protection tours of the following risk-significant plant
    *       RHR Complex, Division I RHRSW Pump Room;
areas:
    *       Hemyc Wrap for the Fire Barrier;
*
    *       Division I, RHR Pump Room;
Condensate Pump Room;
    *       Division II, RHR Pump Room;
*
    *       Main Unit Transformer 2B; and
Standby Gas Treatment, Pipe Room;
    *       Division II Electrical Switchgear Room.
*
    The inspectors verified fire zone conditions were consistent with assumptions in the
Top of Torus;
    licensee's fire hazards analysis. The inspectors walked down fire detection and
*
    suppression equipment, assessed the material condition of fire fighting equipment, and
RHR Complex, Division I RHR;
    evaluated the control of transient combustible materials. In addition, the inspectors
*
    verified fire protection related problems were entered into the corrective action program
RHR Complex, Division I EDG, Switchgear Rooms, Ventilation Rooms;
    with the appropriate significance characterization.
*
    These activities represented eleven routine quarterly fire protection inspection samples.
RHR Complex, Division I RHRSW Pump Room;
   b. Findings
*
    No findings of significance were identified.
Hemyc Wrap for the Fire Barrier;
.2   RHR Complex, Division II EDG, Switchgear and Ventilation Rooms
*
   a. Inspection Scope
Division I, RHR Pump Room;
    The inspectors also conducted fire protection tours of the RHR complex, Division II
*
    EDG, switchgear and ventilation rooms which are risk-significant plant areas.
Division II, RHR Pump Room;
                                              7                                      Enclosure
*
Main Unit Transformer 2B; and
*
Division II Electrical Switchgear Room.
The inspectors verified fire zone conditions were consistent with assumptions in the
licensee's fire hazards analysis. The inspectors walked down fire detection and
suppression equipment, assessed the material condition of fire fighting equipment, and
evaluated the control of transient combustible materials. In addition, the inspectors
verified fire protection related problems were entered into the corrective action program
with the appropriate significance characterization.
These activities represented eleven routine quarterly fire protection inspection samples.
   b.  
Findings
No findings of significance were identified.
.2
RHR Complex, Division II EDG, Switchgear and Ventilation Rooms
   a.
Inspection Scope
The inspectors also conducted fire protection tours of the RHR complex, Division II
EDG, switchgear and ventilation rooms which are risk-significant plant areas.


  The inspectors verified fire zone conditions were consistent with assumptions in the
Enclosure
  licensee's fire hazards analysis. The inspectors walked down fire detection and
8
  suppression equipment, assessed the material condition of fire fighting equipment, and
The inspectors verified fire zone conditions were consistent with assumptions in the
  evaluated the control of transient combustible materials. In addition, the inspectors
licensee's fire hazards analysis. The inspectors walked down fire detection and
  verified fire protection related problems were entered into the corrective action program
suppression equipment, assessed the material condition of fire fighting equipment, and
  with the appropriate significance characterization.
evaluated the control of transient combustible materials. In addition, the inspectors
  These activities represented one routine quarterly fire protection inspection sample.
verified fire protection related problems were entered into the corrective action program
b. Findings
with the appropriate significance characterization.
  Introduction: The inspectors identified an NCV of license condition 2.C(9) having very
These activities represented one routine quarterly fire protection inspection sample.
  low safety significance (Green) for the presence of unauthorized transient combustible
  b.
  materials in the RHR complex.
Findings
  Description: On May 15, 2006, the inspectors identified unauthorized transient
Introduction: The inspectors identified an NCV of license condition 2.C(9) having very
  combustible materials in the RHR complex EDG 12 switchgear room. Specifically, the
low safety significance (Green) for the presence of unauthorized transient combustible
  inspectors identified an office chair and a plastic trash bin approximately half full of
materials in the RHR complex.
  paper secured approximately one foot from panel H21-P351, a safety-related electrical
Description: On May 15, 2006, the inspectors identified unauthorized transient
  panel for EDG 12 room ventilation, and associated cable raceway.
combustible materials in the RHR complex EDG 12 switchgear room. Specifically, the
  Section 9A.1.3.2.e of the UFSAR stated that the fire protection program had a
inspectors identified an office chair and a plastic trash bin approximately half full of
  component to minimize the amount of combustibles to which safety-related areas may
paper secured approximately one foot from panel H21-P351, a safety-related electrical
  be exposed. Procedure MOP11 implemented the fire protection program by prescribing
panel for EDG 12 room ventilation, and associated cable raceway.
  methods for controlling transient combustible material and the location of plant support
Section 9A.1.3.2.e of the UFSAR stated that the fire protection program had a
  equipment. Step 3.5.1 of procedure MOP11 required a Plant Support Equipment
component to minimize the amount of combustibles to which safety-related areas may
  Approval form be obtained before placing any support equipment in the RHR complex.
be exposed. Procedure MOP11 implemented the fire protection program by prescribing
  The procedural requirement existed to ensure the introduction of transient combustible
methods for controlling transient combustible material and the location of plant support
  materials was reviewed by fire protection personnel. However, no Plant Support
equipment. Step 3.5.1 of procedure MOP11 required a Plant Support Equipment
  Equipment Approval form was submitted for the chair and trash bin identified in the
Approval form be obtained before placing any support equipment in the RHR complex.  
  EDG 12 switchgear room within the RHR complex.
The procedural requirement existed to ensure the introduction of transient combustible
  After the inspectors informed the fire protection supervisor of the issue, the fire
materials was reviewed by fire protection personnel. However, no Plant Support
  protection supervisor initiated CARD 06-23388 to initiate corrective actions. Licensee
Equipment Approval form was submitted for the chair and trash bin identified in the
  personnel performed a walkdown of the RHR complex and identified three additional
EDG 12 switchgear room within the RHR complex.
  trash bins and two chairs in other switchgear rooms within the RHR complex. The trash
After the inspectors informed the fire protection supervisor of the issue, the fire
  bins and chairs were removed from the switchgear rooms.
protection supervisor initiated CARD 06-23388 to initiate corrective actions. Licensee
  Analysis: The inspectors determined the licensees failure to properly control transient
personnel performed a walkdown of the RHR complex and identified three additional
  combustibles was a performance deficiency because the licensee is expected to comply
trash bins and two chairs in other switchgear rooms within the RHR complex. The trash
  with their fire hazards analysis and because it was within the licensees ability to foresee
bins and chairs were removed from the switchgear rooms.
  and prevent. The finding was greater than minor in accordance with Inspection Manual
Analysis: The inspectors determined the licensees failure to properly control transient
  Chapter (IMC) 0612, Power Reactor Inspection Reports, Appendix B, Issue
combustibles was a performance deficiency because the licensee is expected to comply
  Disposition Screening, issued September 30, 2005, because the finding affected the
with their fire hazards analysis and because it was within the licensees ability to foresee
  Mitigating Systems Cornerstone attribute for protection against external factors, i.e., fire.
and prevent. The finding was greater than minor in accordance with Inspection Manual
  Specifically, a fire involving the unauthorized transient combustibles could have affected
Chapter (IMC) 0612, Power Reactor Inspection Reports, Appendix B, Issue
  a nearby electrical panel and associated cable raceway containing mitigating system
Disposition Screening, issued September 30, 2005, because the finding affected the
  equipment important to safety. The inspectors identified that a credible fire scenario
Mitigating Systems Cornerstone attribute for protection against external factors, i.e., fire.  
  existed in that equipment important to safety was located within the zone of influence of
Specifically, a fire involving the unauthorized transient combustibles could have affected
                                            8                                      Enclosure
a nearby electrical panel and associated cable raceway containing mitigating system
equipment important to safety. The inspectors identified that a credible fire scenario
existed in that equipment important to safety was located within the zone of influence of


    the unauthorized transient combustible materials as described by Table 2.3.2,
Enclosure
    Calculated Values (in feet) for Use in the Ball and Column Zone of Influence Chart for
9
    Fires in an Open Location Away from Walls of IMC 0609, Appendix F, Fire Protection
the unauthorized transient combustible materials as described by Table 2.3.2,
    Significance Determination Process, issued February 28, 2005.
Calculated Values (in feet) for Use in the Ball and Column Zone of Influence Chart for
    The inspectors completed a significance determination of this issue using IMC 0609,
Fires in an Open Location Away from Walls of IMC 0609, Appendix F, Fire Protection
    Appendix F. The inspectors reviewed IMC 0609, Appendix F, Attachment 2,
Significance Determination Process, issued February 28, 2005.
    Degradation Rating Guidance Specific to Various Fire Protection Program Elements,
The inspectors completed a significance determination of this issue using IMC 0609,
    and determined the unauthorized transient combustible materials represented a low
Appendix F. The inspectors reviewed IMC 0609, Appendix F, Attachment 2,
    degradation rating because the materials would not have ignited from existing sources
Degradation Rating Guidance Specific to Various Fire Protection Program Elements,
    of heat or electrical energy. As such, the finding screened to Green under Question 1 of
and determined the unauthorized transient combustible materials represented a low
    IMC 0609, Appendix F, Task 1.3.1, Qualitative Screening for All Finding Categories,
degradation rating because the materials would not have ignited from existing sources
    and was considered a finding of very low safety significance. The primary cause of this
of heat or electrical energy. As such, the finding screened to Green under Question 1 of
    finding was related to the cross-cutting aspect of problem identification and resolution
IMC 0609, Appendix F, Task 1.3.1, Qualitative Screening for All Finding Categories,
    because the licensees response to several recent instances of unauthorized transient
and was considered a finding of very low safety significance. The primary cause of this
    combustibles was not effective in preventing this instance of unauthorized transient
finding was related to the cross-cutting aspect of problem identification and resolution
    combustibles.
because the licensees response to several recent instances of unauthorized transient
    Enforcement: License condition 2.C.(9) required the licensee to implement and
combustibles was not effective in preventing this instance of unauthorized transient
    maintain in effect all provisions of the approved fire protection program as described in
combustibles.
    the UFSAR. Section 9A.1.3.2.e of the UFSAR stated the fire protection program had a
Enforcement: License condition 2.C.(9) required the licensee to implement and
    component to minimize the amount of combustibles to which safety-related areas may
maintain in effect all provisions of the approved fire protection program as described in
    be exposed. Procedure MOP11 implemented the fire protection program by prescribing
the UFSAR. Section 9A.1.3.2.e of the UFSAR stated the fire protection program had a
    methods for controlling transient combustible material and the location of plant support
component to minimize the amount of combustibles to which safety-related areas may
    equipment. Step 3.5.1 of procedure MOP11 required a Plant Support Equipment
be exposed. Procedure MOP11 implemented the fire protection program by prescribing
    Approval form be obtained before placing any support equipment in the RHR complex, a
methods for controlling transient combustible material and the location of plant support
    safety-related area. Contrary to the above, on May 15, 2006, the inspectors identified
equipment. Step 3.5.1 of procedure MOP11 required a Plant Support Equipment
    support equipment, i.e., a chair and a trash bin, had been placed in the EDG 12
Approval form be obtained before placing any support equipment in the RHR complex, a
    switchgear room within the RHR complex without a Plant Support Equipment Approval
safety-related area. Contrary to the above, on May 15, 2006, the inspectors identified
    form having been obtained. Once identified, the licensee initiated CARD 06-23388,
support equipment, i.e., a chair and a trash bin, had been placed in the EDG 12
    performed a walkdown of the RHR complex, and removed unauthorized chairs and trash
switchgear room within the RHR complex without a Plant Support Equipment Approval
    bins from the switchgear rooms in the RHR complex. Because this violation is of very
form having been obtained. Once identified, the licensee initiated CARD 06-23388,
    low safety significance and because it was entered into the licensees corrective action
performed a walkdown of the RHR complex, and removed unauthorized chairs and trash
    program as CARD 06-23388, this violation is being treated as an NCV, consistent with
bins from the switchgear rooms in the RHR complex. Because this violation is of very
    Section VI.A.1 of the NRC Enforcement Policy: NCV 05000341/2006003-01:
low safety significance and because it was entered into the licensees corrective action  
    Unauthorized Transient Combustibles in Safety-Related Areas.
program as CARD 06-23388, this violation is being treated as an NCV, consistent with
.3   Fire Protection - Drill Observation (71111.05A)
Section VI.A.1 of the NRC Enforcement Policy: NCV 05000341/2006003-01:
   a. Inspection Scope
Unauthorized Transient Combustibles in Safety-Related Areas.
    The inspectors assessed fire brigade performance and the drill evaluators' critique
.3
    during an unannounced fire brigade drill on June 21, 2006. The drill simulated a fire in
Fire Protection - Drill Observation (71111.05A)
    the chemical storage room in the radioactive waste building. The inspectors focused on
   a.
    the command and control of fire brigade activities, fire fighting and communication
Inspection Scope
    practices, material condition and use of fire fighting equipment, and implementation and
The inspectors assessed fire brigade performance and the drill evaluators' critique
    adequacy of pre-planned fire fighting strategies.
during an unannounced fire brigade drill on June 21, 2006. The drill simulated a fire in
                                              9                                    Enclosure
the chemical storage room in the radioactive waste building. The inspectors focused on
the command and control of fire brigade activities, fire fighting and communication
practices, material condition and use of fire fighting equipment, and implementation and
adequacy of pre-planned fire fighting strategies.


  These activities represented one annual fire protection - drill observation inspection
Enclosure
  sample.
10
b. Findings
These activities represented one annual fire protection - drill observation inspection
  Introduction: The inspectors identified a Green NCV of license condition 2.C(9) for the
sample.
  failure to appropriately store chemicals in accordance with the fire hazards analysis.
b.
  Description: The inspectors watched Fire Brigade Drill Scenario Number 6 which
Findings
  involved a simulated fire in the chemical storage room on the first floor of the radioactive
Introduction: The inspectors identified a Green NCV of license condition 2.C(9) for the
  waste building. Firefighters entered the room wearing full protective clothing and
failure to appropriately store chemicals in accordance with the fire hazards analysis.
  positive-pressure, self-contained breathing apparatus. In accordance with fire protection
Description: The inspectors watched Fire Brigade Drill Scenario Number 6 which
  Pre-Plan FP-RDWST, Rev. 4, Radioactive Waste Building Zones 22, 23, 24, and 25, the
involved a simulated fire in the chemical storage room on the first floor of the radioactive
  brigade simulated extinguishing the fire by using a water hose in a fog pattern.
waste building. Firefighters entered the room wearing full protective clothing and
  The inspectors later questioned the adequacy of the fire protection pre-plan because it
positive-pressure, self-contained breathing apparatus. In accordance with fire protection
  did not appear to take into account differences in fire fighting strategies with the various
Pre-Plan FP-RDWST, Rev. 4, Radioactive Waste Building Zones 22, 23, 24, and 25, the
  types of chemicals in the room. After reviewing the list of chemicals in the room against
brigade simulated extinguishing the fire by using a water hose in a fog pattern.
  the fire fighting strategies recommended by NFPA-49, Hazardous Chemicals Data 1994
The inspectors later questioned the adequacy of the fire protection pre-plan because it
  Edition, the inspectors identified four chemicals normally stored in the room where
did not appear to take into account differences in fire fighting strategies with the various
  NFPA-49 recommends using special protective clothing when fighting a fire involving
types of chemicals in the room. After reviewing the list of chemicals in the room against
  those chemicals: monoethylamine solution, sodium hydroxide, potassium hydroxide,
the fire fighting strategies recommended by NFPA-49, Hazardous Chemicals Data 1994
  and sulfuric acid. Additionally, NFPA-49 recommends against the use of water when
Edition, the inspectors identified four chemicals normally stored in the room where
  fighting fires involving sulfuric acid.
NFPA-49 recommends using special protective clothing when fighting a fire involving
  The inspectors reviewed the storage locations of these chemicals and determined they
those chemicals: monoethylamine solution, sodium hydroxide, potassium hydroxide,
  were not segregated in such a manner to ensure a fire in that room did not involve any
and sulfuric acid. Additionally, NFPA-49 recommends against the use of water when
  of those chemicals. Further, the fire protection pre-plan contained no guidance on any
fighting fires involving sulfuric acid.
  special precautions to be followed when fighting a fire involving any of those four
The inspectors reviewed the storage locations of these chemicals and determined they
  chemicals. The inspectors determined it was unreasonable to assume the responding
were not segregated in such a manner to ensure a fire in that room did not involve any
  fire brigade would be able to easily determine what chemicals were on fire given the lack
of those chemicals. Further, the fire protection pre-plan contained no guidance on any
  of labeling and amount of smoke that likely would be present in the room during an
special precautions to be followed when fighting a fire involving any of those four
  actual fire.
chemicals. The inspectors determined it was unreasonable to assume the responding
  The licensees fire hazards analysis, as documented in UFSAR, Section 9A.5.G.3,
fire brigade would be able to easily determine what chemicals were on fire given the lack
  required chemicals be stored in accordance with the guidelines of NFPA-49. Although
of labeling and amount of smoke that likely would be present in the room during an
  the literal storage requirements for these chemicals were generally adhered to, e.g.,
actual fire.
  stored in a cool, dry, ventilated room in metal cabinets, etc., the inspectors determined
The licensees fire hazards analysis, as documented in UFSAR, Section 9A.5.G.3,
  the fire fighting strategies for the four chemicals of interest above were inseparable from
required chemicals be stored in accordance with the guidelines of NFPA-49. Although
  the storage guidelines because the licensee is expected to take all relevant information
the literal storage requirements for these chemicals were generally adhered to, e.g.,
  into account when determining the appropriate chemical storage requirements. For
stored in a cool, dry, ventilated room in metal cabinets, etc., the inspectors determined
  example, although NFPA-49 contained no guidance to store sulfuric acid separately
the fire fighting strategies for the four chemicals of interest above were inseparable from
  from nitric acid, the fact that water is suitable for fires involving nitric acid but not for fires
the storage guidelines because the licensee is expected to take all relevant information
  involving sulfuric acid logically concludes either, a) water should not be used if the
into account when determining the appropriate chemical storage requirements. For
  chemicals are in the same cabinet, b) the sulfuric acid should be stored in a separate
example, although NFPA-49 contained no guidance to store sulfuric acid separately
  container, or c) the quantity of sulfuric acid is controlled sufficiently low so as to not
from nitric acid, the fact that water is suitable for fires involving nitric acid but not for fires
  require segregation; none of which occurred. Likewise, because chemical suits are
involving sulfuric acid logically concludes either, a) water should not be used if the
  recommended for those four chemicals but standard fire fighter turnout gear is suitable
chemicals are in the same cabinet, b) the sulfuric acid should be stored in a separate
  for all other normally stored chemicals in the room, it is reasonable to expect the
container, or c) the quantity of sulfuric acid is controlled sufficiently low so as to not
                                              10                                          Enclosure
require segregation; none of which occurred. Likewise, because chemical suits are
recommended for those four chemicals but standard fire fighter turnout gear is suitable
for all other normally stored chemicals in the room, it is reasonable to expect the


    licensee will take the emergency response personal protective equipment guidelines into
Enclosure
    account when storing chemicals which the licensee also failed to do.
11
    The inspectors questioned the licensee on how chemicals were controlled such that they
licensee will take the emergency response personal protective equipment guidelines into
    did not adversely affect the fire protection strategy and were informed that chemicals
account when storing chemicals which the licensee also failed to do.
    are evaluated based on the effect they would have on the plant but not on the effect
The inspectors questioned the licensee on how chemicals were controlled such that they
    they would have on fire fighting techniques. For example, there were no controls in
did not adversely affect the fire protection strategy and were informed that chemicals
    place to either ensure the fire brigade did not use water on fires involving sulfuric acid or
are evaluated based on the effect they would have on the plant but not on the effect
    to control the amount of sulfuric acid below some threshold to preclude any alteration in
they would have on fire fighting techniques. For example, there were no controls in
    the fire fighting strategy.
place to either ensure the fire brigade did not use water on fires involving sulfuric acid or
    Analysis: The inspectors determined the licensees failure to properly store chemicals in
to control the amount of sulfuric acid below some threshold to preclude any alteration in
    accordance with guidelines contained in NFPA 49 was a performance deficiency
the fire fighting strategy.
    because the licensee is expected to comply with their fire hazards analysis and because
Analysis: The inspectors determined the licensees failure to properly store chemicals in
    it was within the licensees ability to foresee and prevent. The finding is more than
accordance with guidelines contained in NFPA 49 was a performance deficiency
    minor because it represented a programmatic deficiency in the licensees chemical
because the licensee is expected to comply with their fire hazards analysis and because
    control program which affected the ability of the fire brigade to respond to and mitigate
it was within the licensees ability to foresee and prevent. The finding is more than
    the effects of a fire. This finding affected the emergency planning cornerstone because
minor because it represented a programmatic deficiency in the licensees chemical
    it affected the ability of the fire brigade to respond to a fire which could potentially affect
control program which affected the ability of the fire brigade to respond to and mitigate
    the licensees emergency plan.
the effects of a fire. This finding affected the emergency planning cornerstone because
    The finding is not suitable for SDP evaluation, but has been reviewed by NRC
it affected the ability of the fire brigade to respond to a fire which could potentially affect
    management and is determined to be a finding of very low safety significance (Green)
the licensees emergency plan.
    because the quantities of the relevant chemicals were low and the storage location was
The finding is not suitable for SDP evaluation, but has been reviewed by NRC
    sufficiently remote from mitigating equipment.
management and is determined to be a finding of very low safety significance (Green)
    Enforcement: Fermi 2 Facility Operating License NPF-43, condition 2.C(9), required,
because the quantities of the relevant chemicals were low and the storage location was
    in part, that the licensee implement and maintain in effect all provisions of the
sufficiently remote from mitigating equipment.
    approved fire protection program as described in Section 9A of the UFSAR as
Enforcement: Fermi 2 Facility Operating License NPF-43, condition 2.C(9), required,
    amended and approved in the Fermi 2 safety evaluation report through supplement 6.
in part, that the licensee implement and maintain in effect all provisions of the
    UFSAR 9A.5.G.3 required hazardous chemicals be stored in accordance with the
approved fire protection program as described in Section 9A of the UFSAR as
    guidelines of NFPA 49-1994, Hazardous Chemicals Data 1994 Edition. Contrary to
amended and approved in the Fermi 2 safety evaluation report through supplement 6.  
    the above, on June 21, 2006, the licensee failed to utilize the guidelines contained in
UFSAR 9A.5.G.3 required hazardous chemicals be stored in accordance with the
    NFPA 49-1994 when storing chemicals in the radioactive waste building. Because
guidelines of NFPA 49-1994, Hazardous Chemicals Data 1994 Edition. Contrary to
    this violation is of very low safety significance and because it was entered into the
the above, on June 21, 2006, the licensee failed to utilize the guidelines contained in
    licensees corrective action program as CARD 06-24243, this violation is being
NFPA 49-1994 when storing chemicals in the radioactive waste building. Because
    treated as an NCV, consistent with Section VI.A.1 of the NRC Enforcement Policy:
this violation is of very low safety significance and because it was entered into the
    NCV 05000341/2006003-02: Improper Storage of Chemicals Affecting Fire Fighting
licensees corrective action program as CARD 06-24243, this violation is being
    Response.
treated as an NCV, consistent with Section VI.A.1 of the NRC Enforcement Policy:
1R06 Flood Protection (71111.06)
NCV 05000341/2006003-02: Improper Storage of Chemicals Affecting Fire Fighting
a. Inspection Scope
Response.
    The inspectors performed an inspection related to the licensee's precautions to mitigate
1R06
    the risk from internal flooding events. The inspectors performed a walkdown of the
Flood Protection (71111.06)
    following plant areas to assess the adequacy of watertight doors and verify drains and
  a.
    sumps were clear of debris and were operable:
Inspection Scope
                                                11                                    Enclosure
The inspectors performed an inspection related to the licensee's precautions to mitigate
the risk from internal flooding events. The inspectors performed a walkdown of the
following plant areas to assess the adequacy of watertight doors and verify drains and
sumps were clear of debris and were operable:


    *       High Pressure Coolant Injection Pump Room;
Enclosure
    *       Reactor Core Isolation Cooling Pump Room;
12
    *       Division I Core Spray Pump Room;
*
    *       Division II Core Spray Pump Room; and
High Pressure Coolant Injection Pump Room;
    *       Auxiliary Building T Room.
*
    The inspectors also reviewed the work activities associated with internal flooding to
Reactor Core Isolation Cooling Pump Room;
    verify identified problems were being entered into the corrective action program with the
*
    appropriate characterization and significance.
Division I Core Spray Pump Room;
    These activities represented one internal flood protection inspection sample.
*
b. Findings
Division II Core Spray Pump Room; and
    No findings of significance were identified.
*
1R07 Heat Sink Performance (71111.07A)
Auxiliary Building T Room.
a. Inspection Scope
The inspectors also reviewed the work activities associated with internal flooding to
    The inspectors reviewed completed test reports and observed the performance of
verify identified problems were being entered into the corrective action program with the
    inspections for the RHR service water heat exchanger.
appropriate characterization and significance.
    The inspectors selected this heat exchanger because its associated systems were risk
These activities represented one internal flood protection inspection sample.
    significant in the licensee's risk assessment and were required to support the operability
  b.  
    of other risk-significant, safety-related equipment. During these inspections, the
Findings
    inspectors observed the as-found condition of the heat exchanger and verified no
No findings of significance were identified.
    deficiencies existed that would mask degraded performance. The inspectors discussed
1R07
    the as-found condition as well as the historical performance of the heat exchanger with
Heat Sink Performance (71111.07A)
    engineering department personnel and reviewed applicable documents and procedures.
  a.
    In addition, the inspectors verified heat sink problems were entered into the corrective
Inspection Scope
    action program with the appropriate significance characterization, and completed
The inspectors reviewed completed test reports and observed the performance of
    corrective actions were adequate and appropriately implemented.
inspections for the RHR service water heat exchanger.
    These activities represented one heat sink performance inspection sample.
The inspectors selected this heat exchanger because its associated systems were risk
b. Findings
significant in the licensee's risk assessment and were required to support the operability
    No findings of significance were identified.
of other risk-significant, safety-related equipment. During these inspections, the
1R11 Licensed Operator Requalification (71111.11Q)
inspectors observed the as-found condition of the heat exchanger and verified no
a. Inspection Scope
deficiencies existed that would mask degraded performance. The inspectors discussed
    On June 13, 2006, the inspectors observed an operations support crew during the
the as-found condition as well as the historical performance of the heat exchanger with
    annual requalification examination in mitigating the consequences of events in
engineering department personnel and reviewed applicable documents and procedures.
    SS-OP-802-330, Anticipated Transient Without Scram with Small Steam Leak, Rev. 0,
In addition, the inspectors verified heat sink problems were entered into the corrective
    dated January 26, 2006, on the simulator. The inspectors evaluated the following areas:
action program with the appropriate significance characterization, and completed
                                                12                                  Enclosure
corrective actions were adequate and appropriately implemented.
These activities represented one heat sink performance inspection sample.
  b.
Findings
No findings of significance were identified.
1R11
Licensed Operator Requalification (71111.11Q)
  a.
Inspection Scope
On June 13, 2006, the inspectors observed an operations support crew during the
annual requalification examination in mitigating the consequences of events in
SS-OP-802-330, Anticipated Transient Without Scram with Small Steam Leak, Rev. 0,
dated January 26, 2006, on the simulator. The inspectors evaluated the following areas:


    C       licensed operator performance;
Enclosure
    C       crews clarity and formality of communications;
13
    *       ability to take timely actions in the conservative direction;
C
    *       prioritization, interpretation, and verification of annunciator alarms;
licensed operator performance;
    *       correct use and implementation of abnormal and emergency procedures;
C
    C       control board manipulations;
crews clarity and formality of communications;
    C       oversight and direction from supervisors; and
*
    C       ability to identify and implement appropriate TS actions and Emergency Plan
ability to take timely actions in the conservative direction;
            actions and notifications.
*
    The crews performance in these areas was compared to pre-established operator
prioritization, interpretation, and verification of annunciator alarms;
    action expectations and successful critical task completion requirements.
*
    These activities represented one quarterly licensed operator requalification inspection
correct use and implementation of abnormal and emergency procedures;
    sample.
C
b. Findings
control board manipulations;
    No findings of significance were identified.
C
1R12 Maintenance Effectiveness (71111.12Q)
oversight and direction from supervisors; and
a. Inspection Scope
C
    The inspectors evaluated degraded performance issues involving the following three
ability to identify and implement appropriate TS actions and Emergency Plan
    risk-significant systems:
actions and notifications.
    C       Station Blackout Diesel Generators CTG 11-1, 2, 3, 4, and 120 kV switchyard;
The crews performance in these areas was compared to pre-established operator
    C       RHR System A and B; and
action expectations and successful critical task completion requirements.
    C       Molded Case Circuit Breakers.
These activities represented one quarterly licensed operator requalification inspection
    The inspectors assessed performance issues with respect to the reliability, availability,
sample.
    and condition monitoring of the system. Specifically, the inspectors independently
  b.  
    verified the licensee's actions to address system performance or condition problems in
Findings
    terms of the following:
No findings of significance were identified.
    C       implementing appropriate work practices;
1R12
    C       identifying and addressing common cause failures;
Maintenance Effectiveness (71111.12Q)
    C       scoping of systems in accordance with 10 CFR 50.65(b);
  a.  
    C       characterizing system reliability issues;
Inspection Scope
    C       tracking system unavailability;
The inspectors evaluated degraded performance issues involving the following three
    C       trending key parameters (condition monitoring);
risk-significant systems:
    C       ensuring 10 CFR 50.65(a)(1) or (a)(2) classification and/or re-classification; and
C
    C       verifying appropriate performance criteria for systems classified as (a)(2) and/or
Station Blackout Diesel Generators CTG 11-1, 2, 3, 4, and 120 kV switchyard;
            appropriate and adequate goals and corrective actions for systems classified as
C
            (a)(1).
RHR System A and B; and  
    In addition, the inspectors verified maintenance effectiveness issues were entered into
C
    the corrective action program with the appropriate significance characterization.
Molded Case Circuit Breakers.
                                                13                                    Enclosure
The inspectors assessed performance issues with respect to the reliability, availability,
and condition monitoring of the system. Specifically, the inspectors independently
verified the licensee's actions to address system performance or condition problems in
terms of the following:
C
implementing appropriate work practices;
C
identifying and addressing common cause failures;
C
scoping of systems in accordance with 10 CFR 50.65(b);
C
characterizing system reliability issues;
C
tracking system unavailability;
C
trending key parameters (condition monitoring);
C
ensuring 10 CFR 50.65(a)(1) or (a)(2) classification and/or re-classification; and
C
verifying appropriate performance criteria for systems classified as (a)(2) and/or
appropriate and adequate goals and corrective actions for systems classified as
(a)(1).
In addition, the inspectors verified maintenance effectiveness issues were entered into
the corrective action program with the appropriate significance characterization.


    These activities represented three quarterly maintenance effectiveness inspection
Enclosure
    samples.
14
   b. Findings
These activities represented three quarterly maintenance effectiveness inspection
    No findings of significance were identified.
samples.
   b.  
Findings
No findings of significance were identified.
1R13 Maintenance Risk Assessments and Emergent Work Control (71111.13Q)
1R13 Maintenance Risk Assessments and Emergent Work Control (71111.13Q)
.1   Routine Maintenance Risk Assessments
.1
   a. Inspection Scope
Routine Maintenance Risk Assessments
    The inspectors reviewed the licensee's evaluation and management of plant risk for the
   a.  
    maintenance and operational activities affecting risk-significant and safety-related
Inspection Scope
    equipment listed below:
The inspectors reviewed the licensee's evaluation and management of plant risk for the
    *     maintenance risk for week of     April 2, 2006;
maintenance and operational activities affecting risk-significant and safety-related
    *     maintenance risk for week of     April 17, 2006;
equipment listed below:  
    *     maintenance risk for week of     April 30, 2006; and
*
    *     maintenance risk for week of     June 26, 2006.
maintenance risk for week of April 2, 2006;
    These activities were selected based on their potential risk significance relative to the
*
    reactor safety cornerstones. As applicable for each activity, the inspectors reviewed the
maintenance risk for week of April 17, 2006;  
    scope of maintenance work, discussed the results of the assessment with the licensee's
*
    probabilistic risk analyst and/or shift technical advisor, and verified plant conditions were
maintenance risk for week of April 30, 2006; and
    consistent with the risk assessment. The inspectors also reviewed TS requirements and
*
    walked down portions of redundant safety systems, when applicable, to verify risk
maintenance risk for week of June 26, 2006.
    analysis assumptions were valid and applicable requirements were met.
These activities were selected based on their potential risk significance relative to the
    These activities represented four quarterly maintenance risk assessment and
reactor safety cornerstones. As applicable for each activity, the inspectors reviewed the
    emergency work control inspection samples.
scope of maintenance work, discussed the results of the assessment with the licensee's
   b. Findings
probabilistic risk analyst and/or shift technical advisor, and verified plant conditions were
    No findings of significance were identified.
consistent with the risk assessment. The inspectors also reviewed TS requirements and
.2   Inadequate Maintenance Risk Assessment
walked down portions of redundant safety systems, when applicable, to verify risk
   a. Inspection Scope
analysis assumptions were valid and applicable requirements were met.
    The inspectors reviewed the activities surrounding the Division I battery load test
These activities represented four quarterly maintenance risk assessment and
    performed during RF11 to determine if the licensee appropriately considered the risk
emergency work control inspection samples.
    impacts of performing the test. The inspectors interviewed licensee staff, reviewed
   b.  
    documents, and performed walkdowns. The inspectors considered ancillary equipment
Findings
    affected by the test to determine what affect, if any, the test would have on it.
No findings of significance were identified.
    These activities represented one quarterly maintenance risk assessment and
.2
    emergency work control inspection sample.
Inadequate Maintenance Risk Assessment
                                                14                                      Enclosure
   a.
Inspection Scope
The inspectors reviewed the activities surrounding the Division I battery load test
performed during RF11 to determine if the licensee appropriately considered the risk
impacts of performing the test. The inspectors interviewed licensee staff, reviewed
documents, and performed walkdowns. The inspectors considered ancillary equipment
affected by the test to determine what affect, if any, the test would have on it.
These activities represented one quarterly maintenance risk assessment and
emergency work control inspection sample.


b. Findings
Enclosure
  Introduction: The inspectors identified a Green NCV of 10 CFR 50.65(a)(4) for the
15
  failure to perform an adequate risk assessment for the Division I battery load test.
b.
  Description: On April 3, 2006, the inspectors identified a temporary fan installed in the
Findings
  blocked-open doorway to the dc motor control center (DC MCC) area. Upon entering
Introduction: The inspectors identified a Green NCV of 10 CFR 50.65(a)(4) for the
  the room, the inspectors noticed that additional doors inside the DC MCC area leading
failure to perform an adequate risk assessment for the Division I battery load test.
  to each of the reactor protection system motor generator (RPSMG) set rooms were
Description: On April 3, 2006, the inspectors identified a temporary fan installed in the
  open. After questioning why the doors were blocked open and a fan installed, the
blocked-open doorway to the dc motor control center (DC MCC) area. Upon entering
  inspectors learned operators took those actions to provide additional cooling to the
the room, the inspectors noticed that additional doors inside the DC MCC area leading
  RPS MG sets because the Division I 130/260 VDC battery load surveillance test,
to each of the reactor protection system motor generator (RPSMG) set rooms were
  procedure 42.309.05, was in progress.
open. After questioning why the doors were blocked open and a fan installed, the
  Because the air-cooled load bank used for the test was temporarily installed in the
inspectors learned operators took those actions to provide additional cooling to the
  DC MCC area, temperatures in the room started to increase after the test commenced.
RPS MG sets because the Division I 130/260 VDC battery load surveillance test,
  However, two area room coolers were out of service due to a scheduled outage of the
procedure 42.309.05, was in progress.
  GSW system which left the DC MCC, vital battery, battery charger, and RPS MG set
Because the air-cooled load bank used for the test was temporarily installed in the
  rooms with no cooling. In order to help prevent a loss of shutdown cooling, which would
DC MCC area, temperatures in the room started to increase after the test commenced.  
  have occurred had the RPS MG sets tripped, the operators had previously blocked
However, two area room coolers were out of service due to a scheduled outage of the
  opened the doors to the RPS MG set rooms which further increased the temperature in
GSW system which left the DC MCC, vital battery, battery charger, and RPS MG set
  the DC MCC area. Operators then blocked open the double doors to the DC MCC area
rooms with no cooling. In order to help prevent a loss of shutdown cooling, which would
  and installed a large utility fan in the doorway to provide additional cooling to the area.
have occurred had the RPS MG sets tripped, the operators had previously blocked
  The test was successfully completed, temperatures dropped, and the fan was removed.
opened the doors to the RPS MG set rooms which further increased the temperature in
  The outage risk associated with this test did not consider the effects it would have on
the DC MCC area. Operators then blocked open the double doors to the DC MCC area
  the key safety function of maintaining decay heat available due to the additional heat
and installed a large utility fan in the doorway to provide additional cooling to the area.  
  from the load bank with no room cooling. Moreover, the outage risk associated with the
The test was successfully completed, temperatures dropped, and the fan was removed.
  GSW outage assumed that the RPS MG sets would not be running. Consequently,
The outage risk associated with this test did not consider the effects it would have on
  prudent risk management actions were not developed prior to performing the battery
the key safety function of maintaining decay heat available due to the additional heat
  load test. However, because operators installed a fan in the open doorway early
from the load bank with no room cooling. Moreover, the outage risk associated with the
  enough into the test, shutdown cooling remained in operation.
GSW outage assumed that the RPS MG sets would not be running. Consequently,
  Analysis: The inspectors determined the failure to perform an adequate risk analysis of
prudent risk management actions were not developed prior to performing the battery
  maintenance activities prior to performing maintenance was a performance deficiency
load test. However, because operators installed a fan in the open doorway early
  because the licensee is expected to comply with the requirements of the maintenance
enough into the test, shutdown cooling remained in operation.
  rule. This finding is more than minor because the licensees risk assessment failed to
Analysis: The inspectors determined the failure to perform an adequate risk analysis of
  consider maintenance activities that could increase the likelihood of an initiating event,
maintenance activities prior to performing maintenance was a performance deficiency
  specifically a loss of shutdown cooling. In addition, this finding affected the initiating
because the licensee is expected to comply with the requirements of the maintenance
  event cornerstone because it is associated with an increase in the likelihood of an
rule. This finding is more than minor because the licensees risk assessment failed to
  initiating event. The inspectors utilized the maintenance risk and shutdown risk SDP to
consider maintenance activities that could increase the likelihood of an initiating event,
  assess the risk of this finding. The finding is of very low safety significance because the
specifically a loss of shutdown cooling. In addition, this finding affected the initiating
  finding did not affect the ability of operators to recover from a loss of shutdown cooling
event cornerstone because it is associated with an increase in the likelihood of an
  had it occurred. The inspectors determined the cause of this finding impacted the
initiating event. The inspectors utilized the maintenance risk and shutdown risk SDP to
  Human Performance cross-cutting area because the cause of the inadequate risk
assess the risk of this finding. The finding is of very low safety significance because the
  assessment was due to a personnel error.
finding did not affect the ability of operators to recover from a loss of shutdown cooling
  Enforcement: 10 CFR 50.65(a)(4) requires, in part, that before performing
had it occurred. The inspectors determined the cause of this finding impacted the
  maintenance activities, the licensee shall assess and manage the increase in risk
Human Performance cross-cutting area because the cause of the inadequate risk
                                              15                                      Enclosure
assessment was due to a personnel error.
Enforcement: 10 CFR 50.65(a)(4) requires, in part, that before performing
maintenance activities, the licensee shall assess and manage the increase in risk


    that may result from the proposed maintenance activities. Contrary to the above,
Enclosure
    beginning on April 1, 2006, and continuing through April 6, 2006, the licensee
16
    performed surveillance procedure 42.309.05 without adequately assessing and
that may result from the proposed maintenance activities. Contrary to the above,
    managing the increase in risk prior to performing the activity. Because this violation is
beginning on April 1, 2006, and continuing through April 6, 2006, the licensee
    of very low safety significance and because it was entered into the licensees corrective
performed surveillance procedure 42.309.05 without adequately assessing and
    action program as CARD 06-21892 and 06-24495, this violation is being treated as an
managing the increase in risk prior to performing the activity. Because this violation is
    NCV, consistent with Section VI.A.1 of the NRC Enforcement Policy:
of very low safety significance and because it was entered into the licensees corrective
    NCV 05000341/2006003-03: Inadequate Maintenance Risk Assessment.
action program as CARD 06-21892 and 06-24495, this violation is being treated as an
1R14 Personnel Performance During Non-Routine Plant Evolutions and Events (71111.14)
NCV, consistent with Section VI.A.1 of the NRC Enforcement Policy:
   a. Inspection Scope
NCV 05000341/2006003-03: Inadequate Maintenance Risk Assessment.
    The inspectors reviewed the licensees actions in response to the following non-routine
1R14
    events to ensure the licensee took appropriate actions in accordance with licensee
Personnel Performance During Non-Routine Plant Evolutions and Events (71111.14)
    procedures:
   a.
    *       unplanned reactor building contamination, CARD 06-21534;
Inspection Scope
    *       control rod position indication malfunction, CARD 06-23491 & 06-23489;
The inspectors reviewed the licensees actions in response to the following non-routine
    *       main turbine bypass valves opened at power, CARD 06-24113; and
events to ensure the licensee took appropriate actions in accordance with licensee
    *       mode 5 reactor scram during installation of shorting links, CARD 06-23588.
procedures:
    The inspectors reviewed operator logs, procedures, corrective action documents, other
*
    documents, and interviewed personnel. The inspectors also evaluated the licensees
unplanned reactor building contamination, CARD 06-21534;
    operational decision making involved with these non-routine events.
*
    These activities represented four inspection samples.
control rod position indication malfunction, CARD 06-23491 & 06-23489;
   b. Findings
*
    No findings of significance were identified.
main turbine bypass valves opened at power, CARD 06-24113; and
1R15 Operability Evaluations (71111.15)
*
  .1 Routine Review of Operability Evaluations
mode 5 reactor scram during installation of shorting links, CARD 06-23588.
   a. Inspection Scope
The inspectors reviewed operator logs, procedures, corrective action documents, other
    The inspectors reviewed the following documents to ensure the identified condition did
documents, and interviewed personnel. The inspectors also evaluated the licensees
    not render the involved equipment inoperable or result in an unrecognized increase in
operational decision making involved with these non-routine events.  
    plant risk, and the licensee appropriately applied TS limitations and appropriately
These activities represented four inspection samples.  
    returned the affected equipment to an operable status:
   b.  
    *       CARD 06-23114, Motor Operator Valve Motor Replacement for RHR Shutdown
Findings
            Cooling Inboard Suction Bypass Valve; and
No findings of significance were identified.
    *       CARD 06-23898, Division II Emergency Equipment Cooling Water Makeup
1R15
            Pump In-Service Test Flow Unattainable.
Operability Evaluations (71111.15)
    These activities represented two operability evaluation inspection samples.
  .1  
                                              16                                    Enclosure
Routine Review of Operability Evaluations
   a.  
Inspection Scope
The inspectors reviewed the following documents to ensure the identified condition did
not render the involved equipment inoperable or result in an unrecognized increase in
plant risk, and the licensee appropriately applied TS limitations and appropriately
returned the affected equipment to an operable status:
*
CARD 06-23114, Motor Operator Valve Motor Replacement for RHR Shutdown
Cooling Inboard Suction Bypass Valve; and
*
CARD 06-23898, Division II Emergency Equipment Cooling Water Makeup
Pump In-Service Test Flow Unattainable.
These activities represented two operability evaluation inspection samples.


b. Findings
Enclosure
    No findings of significance were identified.
17
.2 Standby Liquid Control Operability During Air Sparging Operations
  b.  
a. Inspection Scope
Findings
    The inspectors reviewed the licensees practice of placing an air sparge on the SLC tank
No findings of significance were identified.
    to determine if system operability was justified. The inspectors reviewed previous
.2  
    engineering evaluations to determine the technical adequacy of the conclusions. The
Standby Liquid Control Operability During Air Sparging Operations
    inspectors reviewed operator logs, TS, design basis documents, UFSAR, and other
  a.
    documents. The inspectors interviewed operators, engineers, and other licensee staff.
Inspection Scope
    These activities represented one operability evaluation inspection sample.
The inspectors reviewed the licensees practice of placing an air sparge on the SLC tank
b. Findings
to determine if system operability was justified. The inspectors reviewed previous
    Introduction: The inspectors identified a Green NCV of TS for the SLC system being
engineering evaluations to determine the technical adequacy of the conclusions. The
    inoperable for longer than the action time to be in hot shutdown with both SLC
inspectors reviewed operator logs, TS, design basis documents, UFSAR, and other
    subsystems inoperable.
documents. The inspectors interviewed operators, engineers, and other licensee staff.
    Description: In April 1999, the licensee reviewed an operating experience report issued
These activities represented one operability evaluation inspection sample.
    by another licensee discussing the inoperability of the SLC system during air sparging
b.
    activities. Air sparging the SLC tank was done to facilitate mixing of the sodium
Findings
    pentaborate in the tank and was performed prior to the monthly chemistry analysis and
Introduction: The inspectors identified a Green NCV of TS for the SLC system being
    after any chemical addition to the tank. The air sparge header was located near the
inoperable for longer than the action time to be in hot shutdown with both SLC
    bottom of the tank in proximity to the SLC pump suction line. The concern was that if
subsystems inoperable.
    the pumps were operating while the air sparge was operating, air could be drawn into
Description: In April 1999, the licensee reviewed an operating experience report issued
    the pumps and compromise their ability to perform their design function. The licensee
by another licensee discussing the inoperability of the SLC system during air sparging
    initiated CARD 99-13240 to evaluate the applicability of the issue to Fermi.
activities. Air sparging the SLC tank was done to facilitate mixing of the sodium
    The licensee determined that although pump performance would be impacted if the
pentaborate in the tank and was performed prior to the monthly chemistry analysis and
    pumps were required while an SLC tank air sparge was in progress, the pumps
after any chemical addition to the tank. The air sparge header was located near the
    remained operable. Based on input from the pump vendor, the licensee concluded that
bottom of the tank in proximity to the SLC pump suction line. The concern was that if
    entrained air in the pumped water would cause increased pump vibration and a
the pumps were operating while the air sparge was operating, air could be drawn into
    negligible reduction in delivered flow rate. Because the vendor stated the increased
the pumps and compromise their ability to perform their design function. The licensee
    vibration would only affect long-term pump reliability, the licensee concluded that
initiated CARD 99-13240 to evaluate the applicability of the issue to Fermi.
    long-term pump degradation was not a concern because SLC had a 2 hour mission
The licensee determined that although pump performance would be impacted if the
    time.
pumps were required while an SLC tank air sparge was in progress, the pumps
    In an effort to lessen the probability of requiring the SLC pumps during an actual event
remained operable. Based on input from the pump vendor, the licensee concluded that
    while the air sparge was operating, the licensee identified the need to revise the system
entrained air in the pumped water would cause increased pump vibration and a
    operating procedures to minimize duration of sparge operations from hours to minutes.
negligible reduction in delivered flow rate. Because the vendor stated the increased
    The action to revise procedure 23.149, Standby Liquid Control System, was originally
vibration would only affect long-term pump reliability, the licensee concluded that
    due on June 30, 1999.
long-term pump degradation was not a concern because SLC had a 2 hour mission
    The inspectors reviewed the licensees evaluation and noted the CARD did not contain
time.
    either any documentation from the vendor or any attempt to quantify the reduction in
In an effort to lessen the probability of requiring the SLC pumps during an actual event
                                              17                                  Enclosure
while the air sparge was operating, the licensee identified the need to revise the system
operating procedures to minimize duration of sparge operations from hours to minutes.  
The action to revise procedure 23.149, Standby Liquid Control System, was originally
due on June 30, 1999.
The inspectors reviewed the licensees evaluation and noted the CARD did not contain
either any documentation from the vendor or any attempt to quantify the reduction in


flow rate to ensure the minimum required flow was maintained. The inspectors asked
Enclosure
18
flow rate to ensure the minimum required flow was maintained. The inspectors asked
the licensee for the vendors recommendations in writing but were later told the pump
the licensee for the vendors recommendations in writing but were later told the pump
vendor declined to support their previous conclusion in writing. The inspectors were
vendor declined to support their previous conclusion in writing. The inspectors were
concerned that if the pump vendor was unwilling to state in writing that the pumps would
concerned that if the pump vendor was unwilling to state in writing that the pumps would
operate for at least 2 hours during sparging, then pump operability was not justified.
operate for at least 2 hours during sparging, then pump operability was not justified.
The inspectors brought their concern to the licensee who entered the issue into their
The inspectors brought their concern to the licensee who entered the issue into their
corrective action program as CARD 06-23785 on June 1, 2006. After further review, the
corrective action program as CARD 06-23785 on June 1, 2006. After further review, the
licensee concluded that SLC operability during sparging could not be supported and
licensee concluded that SLC operability during sparging could not be supported and
revised procedure 23.149 accordingly. Upon review of control room logs, the inspectors
revised procedure 23.149 accordingly. Upon review of control room logs, the inspectors
determined that although the licensee significantly reduced the total sparging time since
determined that although the licensee significantly reduced the total sparging time since
1999, the tank was air sparged for 21 hours on August 24, 1999, which exceeded the
1999, the tank was air sparged for 21 hours on August 24, 1999, which exceeded the
time to be in hot shutdown of 20 hours with both SLC subsystems inoperable while in
time to be in hot shutdown of 20 hours with both SLC subsystems inoperable while in
Mode 1 or 2. In addition, the inspectors concluded the maximum unavailability in any
Mode 1 or 2. In addition, the inspectors concluded the maximum unavailability in any
1-year period after identification of the issue in 1999 was approximately 90 hours.
1-year period after identification of the issue in 1999 was approximately 90 hours.
Analysis: The inspectors determined the licensees failure to appropriately evaluate
Analysis: The inspectors determined the licensees failure to appropriately evaluate
SLC operability during sparging operations was a performance deficiency because the
SLC operability during sparging operations was a performance deficiency because the
licensee is expected to adequately evaluate issues that affect the operability of TS
licensee is expected to adequately evaluate issues that affect the operability of TS
equipment and because it was within the licensees ability to foresee and prevent. The
equipment and because it was within the licensees ability to foresee and prevent. The
finding is more than minor because it affected the equipment performance attribute of
finding is more than minor because it affected the equipment performance attribute of
the reactor safety cornerstone objective of ensuring the availability, reliability, and
the reactor safety cornerstone objective of ensuring the availability, reliability, and
capability of mitigating equipment to respond to initiating events to prevent undesirable
capability of mitigating equipment to respond to initiating events to prevent undesirable
consequences.
consequences.
The inspectors assessed the finding using the SDP. Because the inspectors
The inspectors assessed the finding using the SDP. Because the inspectors
considered this finding to represent an actual loss of a safety function of SLC, the
considered this finding to represent an actual loss of a safety function of SLC, the
inspectors performed a phase 2 SDP analysis. A phase 3 analysis was subsequently
inspectors performed a phase 2 SDP analysis. A phase 3 analysis was subsequently
performed by the senior reactor analyst (SRA). The SRA performed the risk evaluation
performed by the senior reactor analyst (SRA). The SRA performed the risk evaluation
using the Fermi Standardized Plant Analysis Risk (SPAR) Model, Level 1, Revision 3P,
using the Fermi Standardized Plant Analysis Risk (SPAR) Model, Level 1, Revision 3P,
Change 3.21, created October 2005. The SRA ran the SPAR model assuming common
Change 3.21, created October 2005. The SRA ran the SPAR model assuming common
cause failure of both SLC pumps, with an exposure time of 90 hours. Using the above
cause failure of both SLC pumps, with an exposure time of 90 hours. Using the above
information the SRA obtained a change in core damage frequency (CDF) of 3.1E-8
information the SRA obtained a change in core damage frequency (CDF) of 3.1E-8
(Green) for internal events. The dominant sequences involved a failure of the reactor to
(Green) for internal events. The dominant sequences involved a failure of the reactor to
scram after a transient, loss of condenser heat sink, and loss of main feedwater, and
scram after a transient, loss of condenser heat sink, and loss of main feedwater, and
failure of the SLC system.
failure of the SLC system.  
Anticipated transient without scram events are not assumed to be caused by external
Anticipated transient without scram events are not assumed to be caused by external
events and, therefore, the risk contribution from external events is insignificant.
events and, therefore, the risk contribution from external events is insignificant.  
Similarly, because the internal events CDF is less than 1E-7, large early release
Similarly, because the internal events CDF is less than 1E-7, large early release
frequency (LERF) is not significant per IMC 0609, Appendix H. The SRA concluded
frequency (LERF) is not significant per IMC 0609, Appendix H. The SRA concluded
the total CDF considering internal events, external events, and LERF is estimated at
the total CDF considering internal events, external events, and LERF is estimated at
3.1E-8 (Green).
3.1E-8 (Green).
Enforcement: Technical Specification 3.1.5.a.2, Amendment 38, required that while in
Enforcement: Technical Specification 3.1.5.a.2, Amendment 38, required that while in
Modes 1 and 2, with the SLC system otherwise inoperable, the licensee must restore
Modes 1 and 2, with the SLC system otherwise inoperable, the licensee must restore
the system to operable status within 8 hours or be in at least hot shutdown within the
the system to operable status within 8 hours or be in at least hot shutdown within the
next 12 hours and was in effect on August 24 and 25, 1999. Contrary to the above,
next 12 hours and was in effect on August 24 and 25, 1999. Contrary to the above,
beginning on August 24, 1999, and continuing until August 25, 1999, while in Modes 1
beginning on August 24, 1999, and continuing until August 25, 1999, while in Modes 1
                                          18                                        Enclosure


    and 2, the SLC system was inoperable for 21 hours while the SLC tank was being air
Enclosure
    sparged; therefore, on August 25, 1999, with the SLC system inoperable for greater
19
    than 20 hours, the plant was not in at least hot shutdown. Because this violation is of
and 2, the SLC system was inoperable for 21 hours while the SLC tank was being air
    very low safety significance and because it was entered into the licensees corrective
sparged; therefore, on August 25, 1999, with the SLC system inoperable for greater
    action program as CARD 06-23785, this finding is being treated as an NCV, consistent
than 20 hours, the plant was not in at least hot shutdown. Because this violation is of
    with Section VI.A.1 of the NRC Enforcement Policy: NCV 05000341/2006003-04:
very low safety significance and because it was entered into the licensees corrective
    Improper Evaluation of Standby Liquid Control Operability During Tank Sparging.
action program as CARD 06-23785, this finding is being treated as an NCV, consistent
.3 Inappropriate Use of Risk in Operability Evaluations
with Section VI.A.1 of the NRC Enforcement Policy: NCV 05000341/2006003-04:  
a. Inspection Scope
Improper Evaluation of Standby Liquid Control Operability During Tank Sparging.
    The inspectors reviewed CARD 06-23913 to ensure that the identified condition did not
.3
    render the involved equipment inoperable or result in an unrecognized increase in plant
Inappropriate Use of Risk in Operability Evaluations
    risk and that the licensee appropriately applied TS limitations and appropriately returned
  a.  
    the affected equipment to an operable status.
Inspection Scope
    These activities represented one operability evaluation inspection sample.
The inspectors reviewed CARD 06-23913 to ensure that the identified condition did not
    Introduction: The inspectors identified an Unresolved Item (URI) when the licensee
render the involved equipment inoperable or result in an unrecognized increase in plant
    removed pipe insulation, credited for environmental qualification of nearby equipment,
risk and that the licensee appropriately applied TS limitations and appropriately returned
    while at power without an adequate engineering evaluation.
the affected equipment to an operable status.
    Description: On June 8, 2006, the licensee initiated CARD 06-23913 to request a work
These activities represented one operability evaluation inspection sample.
    request to replace contaminated insulation on the suction and discharge pipe for the B
Introduction: The inspectors identified an Unresolved Item (URI) when the licensee
    RHR pump. As a result, Work Request (WR) 000Z062027 was released and work
removed pipe insulation, credited for environmental qualification of nearby equipment,
    began on June 13, 2006. While performing a plant tour on June 15, 2006, the
while at power without an adequate engineering evaluation.
    inspectors identified the insulation was missing from the suction pipe for the B RHR
Description: On June 8, 2006, the licensee initiated CARD 06-23913 to request a work
    pump and questioned the licensee if the insulation removal had an approved
request to replace contaminated insulation on the suction and discharge pipe for the B
    engineering evaluation. Because the equipment was in a potentially harsh environment,
RHR pump. As a result, Work Request (WR) 000Z062027 was released and work
    the uninsulated pipe would increase the temperature profile of the room during accident
began on June 13, 2006. While performing a plant tour on June 15, 2006, the
    conditions which could affect the environmental qualification of electrical equipment in
inspectors identified the insulation was missing from the suction pipe for the B RHR
    the room. The licensee stated the evaluation was documented in CARD 06-23913 and
pump and questioned the licensee if the insulation removal had an approved
    concluded that removing the insulation while at power was acceptable.
engineering evaluation. Because the equipment was in a potentially harsh environment,
    The inspectors reviewed the subject evaluation and became concerned that one of the
the uninsulated pipe would increase the temperature profile of the room during accident
    assumptions for the evaluation was that an accident was not considered as credible
conditions which could affect the environmental qualification of electrical equipment in
    during the period of time the insulation was to be removed. Upon further review, the
the room. The licensee stated the evaluation was documented in CARD 06-23913 and
    inspectors learned the licensee used non-accident heat loads to determine the
concluded that removing the insulation while at power was acceptable.
    environmental effects of removing the insulation. The licensees justification was that if
The inspectors reviewed the subject evaluation and became concerned that one of the
    the total time the insulation was removed was less than 168 hours, then the probability
assumptions for the evaluation was that an accident was not considered as credible
    of either a high energy line break or loss of coolant accident was negligible and, hence,
during the period of time the insulation was to be removed. Upon further review, the
    did not need to be assumed to occur.
inspectors learned the licensee used non-accident heat loads to determine the
    The definition of operability stated, however, the equipment must be capable of
environmental effects of removing the insulation. The licensees justification was that if
    performing its specified function(s). The inherent assumption was the occurrence,
the total time the insulation was removed was less than 168 hours, then the probability
    conditions, or event would exist and the safety function could be performed. Therefore,
of either a high energy line break or loss of coolant accident was negligible and, hence,
                                            19                                    Enclosure
did not need to be assumed to occur.
The definition of operability stated, however, the equipment must be capable of
performing its specified function(s). The inherent assumption was the occurrence,
conditions, or event would exist and the safety function could be performed. Therefore,  


    the inspectors concluded the use of probabilities of the occurrence of accidents while
Enclosure
    the insulation was removed was an unacceptable assumption in the subsequent
20
    operability evaluation.
the inspectors concluded the use of probabilities of the occurrence of accidents while
    While reviewing this evaluation, the inspectors discovered the licensee used the
the insulation was removed was an unacceptable assumption in the subsequent
    same method of evaluating on-line insulation removal since at least September 20,
operability evaluation.
    2001, and found five additional CARDs where the licensee approved removing
While reviewing this evaluation, the inspectors discovered the licensee used the
    insulation from equipment in potentially harsh areas while at power, likewise with
same method of evaluating on-line insulation removal since at least September 20,
    unacceptable evaluations. Because the extent of condition of this issue is potentially
2001, and found five additional CARDs where the licensee approved removing
    significant and could extend to work other than on-line insulation removal, this item is
insulation from equipment in potentially harsh areas while at power, likewise with
    unresolved pending the inspectors review of the licensees full extent of condition
unacceptable evaluations. Because the extent of condition of this issue is potentially
    review and subsequent risk evaluation and is identified as Unresolved Item
significant and could extend to work other than on-line insulation removal, this item is
    (URI) 05000341/2006003-05: Inappropriate Use of Risk in Operability Evaluations.
unresolved pending the inspectors review of the licensees full extent of condition
1R19 Post-Maintenance Testing (71111.19)
review and subsequent risk evaluation and is identified as Unresolved Item
a. Inspection Scope
(URI) 05000341/2006003-05: Inappropriate Use of Risk in Operability Evaluations.
    The inspectors reviewed post-maintenance testing (PMT) activities associated with the
1R19
    following scheduled maintenance:
Post-Maintenance Testing (71111.19)
    *       Division I Switchyard Modifications, EDP 31880;
  a.
    *       Feedwater Check Valve PMT, WR T210040100;
Inspection Scope
    *       Drywell Cooler Number 4 Replacement, WR 000Z052131;
The inspectors reviewed post-maintenance testing (PMT) activities associated with the
    *       Reactor Core Isolation Cooling PMT;
following scheduled maintenance:
    *       Reactor Recirculation Pump Discharge Valve B310SF031A, Stem Replacement,
*
            WR 000Z050487;
Division I Switchyard Modifications, EDP 31880;
    *       Main Steam Isolation Valve (MSIV), Limit Switch Replacement; and
*
    *       WR 000Z060156, Replace Control Rod Drive Pump Inboard Bearing Oil Level
Feedwater Check Valve PMT, WR T210040100;
            Sight glass.
*
    The inspectors reviewed the scope of the work performed and evaluated the adequacy
Drywell Cooler Number 4 Replacement, WR 000Z052131;
    of the specified PMT. The inspectors verified the PMT was performed in accordance
*
    with approved procedures, the procedures clearly stated acceptance criteria, and the
Reactor Core Isolation Cooling PMT;
    acceptance criteria were met. The inspectors interviewed operations, maintenance, and
*
    engineering department personnel and reviewed the completed PMT documentation.
Reactor Recirculation Pump Discharge Valve B310SF031A, Stem Replacement,
    In addition, the inspectors verified PMT problems were entered into the corrective action
WR 000Z050487;
    program with the appropriate significance characterization.
*
    These activities represented seven PMT inspection samples.
Main Steam Isolation Valve (MSIV), Limit Switch Replacement; and  
b.  Findings
*
    No findings of significance were identified.
WR 000Z060156, Replace Control Rod Drive Pump Inboard Bearing Oil Level
                                              20                                    Enclosure
Sight glass.
The inspectors reviewed the scope of the work performed and evaluated the adequacy
of the specified PMT. The inspectors verified the PMT was performed in accordance
with approved procedures, the procedures clearly stated acceptance criteria, and the
acceptance criteria were met. The inspectors interviewed operations, maintenance, and
engineering department personnel and reviewed the completed PMT documentation.
In addition, the inspectors verified PMT problems were entered into the corrective action
program with the appropriate significance characterization.
These activities represented seven PMT inspection samples.
  b.   
Findings
No findings of significance were identified.


1R20 Refueling and Outage Activities (71111.20)
Enclosure
.1 Routine Refueling Outage Inspection Activities
21
a. Inspection Scope
1R20
    The inspectors observed the licensees performance during RF11, which was in
Refueling and Outage Activities (71111.20)
    progress at the beginning of this inspection and concluded on May 5, 2006.
  .1
    This inspection consisted of a review of the licensees outage schedule, safe shutdown
Routine Refueling Outage Inspection Activities
    plan and administrative procedures governing the outage, periodic observations of
  a.
    equipment alignment, and plant and control room outage activities. Specifically, the
Inspection Scope
    inspectors determined whether the licensee effectively managed elements of shutdown
The inspectors observed the licensees performance during RF11, which was in
    risk pertaining to reactivity control, decay heat removal, inventory control, electrical
progress at the beginning of this inspection and concluded on May 5, 2006.
    power control, and containment integrity.
This inspection consisted of a review of the licensees outage schedule, safe shutdown
    The inspectors performed the following activities daily, during the outage:
plan and administrative procedures governing the outage, periodic observations of
    *       attended control room operator and outage management turnover meetings to
equipment alignment, and plant and control room outage activities. Specifically, the
              verify the current shutdown risk status was well understood and communicated;
inspectors determined whether the licensee effectively managed elements of shutdown
    *       performed walkdowns of the main control room to observe the alignment of
risk pertaining to reactivity control, decay heat removal, inventory control, electrical
              systems important to shutdown risk;
power control, and containment integrity.  
    *       observed the operability of reactor coolant system (RCS) instrumentation and
The inspectors performed the following activities daily, during the outage:
              compared channels and trains against one another;
*
    *       performed walkdowns of the turbine, auxiliary, and reactor buildings and the
attended control room operator and outage management turnover meetings to
              drywell to observe ongoing work activities, to ensure work activities were
verify the current shutdown risk status was well understood and communicated;
              performed in accordance with plant procedures, and to verify procedural
*
              requirements regarding fire protection, foreign material exclusion, and the
performed walkdowns of the main control room to observe the alignment of  
              storage of equipment near safety-related structures, systems, and components
systems important to shutdown risk;
              were maintained;
*
    *       verified the licensee maintained secondary containment in accordance with TS
observed the operability of reactor coolant system (RCS) instrumentation and
              requirements; and
compared channels and trains against one another;
    *       reviewed selected issues the licensee entered into its corrective action program
*
              to verify identified problems were being entered into the program with the
performed walkdowns of the turbine, auxiliary, and reactor buildings and the
              appropriate characterization and significance.
drywell to observe ongoing work activities, to ensure work activities were
    Additionally, the inspectors performed the following specific activities:
performed in accordance with plant procedures, and to verify procedural
    *       monitored refueling activities to verify the licensee adhered to established
requirements regarding fire protection, foreign material exclusion, and the
              procedures and TS requirements for handling of irradiated fuel;
storage of equipment near safety-related structures, systems, and components
    *       performed drywell closeout;
were maintained;
    *       verified shutdown cooling tagouts;
*
    *       verified completion of restart restraint items; and
verified the licensee maintained secondary containment in accordance with TS
    *       observed control rod withdrawal to criticality and portions of the plant power
requirements; and
              ascension.
*
    In particular, the inspectors reviewed the licensees restart restraint process and verified
reviewed selected issues the licensee entered into its corrective action program
    the closure of selected issues. Documents reviewed during these inspection activities
to verify identified problems were being entered into the program with the
    are listed at the end of this report.
appropriate characterization and significance.
                                                21                                      Enclosure
Additionally, the inspectors performed the following specific activities:
*
monitored refueling activities to verify the licensee adhered to established
procedures and TS requirements for handling of irradiated fuel;
*
performed drywell closeout;
*
verified shutdown cooling tagouts;
*
verified completion of restart restraint items; and
*
observed control rod withdrawal to criticality and portions of the plant power
ascension.  
In particular, the inspectors reviewed the licensees restart restraint process and verified
the closure of selected issues. Documents reviewed during these inspection activities
are listed at the end of this report.


  Because inspection activities for this refueling outage constituted one inspection sample
Enclosure
  in Inspection Report 05000341/2006002, and since only one sample is counted per
22
  outage, the inspection activities for this inspection period do not constitute an additional
Because inspection activities for this refueling outage constituted one inspection sample
  refueling and outage inspection sample.
in Inspection Report 05000341/2006002, and since only one sample is counted per
b. Findings
outage, the inspection activities for this inspection period do not constitute an additional
  Introduction: The inspectors identified a Green NCV of Technical Specification 5.4.1.a,
refueling and outage inspection sample.
  for the failure to adequately control the modification of the ventilation equipment used to
b.  
  vent airborne radioactive particulate to the refuel floor during reactor vessel floodup.
Findings
  Description: At 1450, on March 26, 2006, operators initiated core spray at approximately
Introduction: The inspectors identified a Green NCV of Technical Specification 5.4.1.a,
  3000 gpm to raise reactor water level, to permit removal of the reactor vessel head. The
for the failure to adequately control the modification of the ventilation equipment used to
  reactor vessel head vent pipe had been disconnected, to permit installation of a
vent airborne radioactive particulate to the refuel floor during reactor vessel floodup.
  ventilation unit for the venting of gases to the refuel floor. The ventilation unit consisted
Description: At 1450, on March 26, 2006, operators initiated core spray at approximately
  of a nominal 3600 scfm fan, a charcoal filter, and a HEPA particulate filter. Neither filter
3000 gpm to raise reactor water level, to permit removal of the reactor vessel head. The
  had been recently tested. The ventilation unit was configured with two hoses placed to
reactor vessel head vent pipe had been disconnected, to permit installation of a
  take suction close to the reactor vessel head vent. The exhaust of the ventilation unit
ventilation unit for the venting of gases to the refuel floor. The ventilation unit consisted
  ran to a point below an intake for the Standby Gas Treatment System (SGTS), to permit
of a nominal 3600 scfm fan, a charcoal filter, and a HEPA particulate filter. Neither filter
  capture of the exhaust by the SGTS.
had been recently tested. The ventilation unit was configured with two hoses placed to
  At approximately 1500, the ventilation unit intake hoses were observed being pushed
take suction close to the reactor vessel head vent. The exhaust of the ventilation unit
  away from the reactor vessel head vent, due to flow from the vent. Core spray was shut
ran to a point below an intake for the Standby Gas Treatment System (SGTS), to permit
  down at 1502 and at 1504 visible moisture was seen being emitted from the vent. A
capture of the exhaust by the SGTS.
  continuous air monitor on the refuel floor alarmed at 1510 and RP ordered the
At approximately 1500, the ventilation unit intake hoses were observed being pushed
  evacuation of all but essential personnel from the refuel floor. By 1525 all personnel
away from the reactor vessel head vent, due to flow from the vent. Core spray was shut
  were removed from the floor and shortly after this, the entire reactor building was
down at 1502 and at 1504 visible moisture was seen being emitted from the vent. A
  evacuated due to the spread of contamination. Decontamination of several workers was
continuous air monitor on the refuel floor alarmed at 1510 and RP ordered the
  required. Twenty-eight workers were whole body counted, with 26 showing uptakes of
evacuation of all but essential personnel from the refuel floor. By 1525 all personnel
  varying levels of Co-60, Co-58, and Mn-54.
were removed from the floor and shortly after this, the entire reactor building was
  There were three conditions that contributed to the cause of the event. First of all,
evacuated due to the spread of contamination. Decontamination of several workers was
  coolant activity levels were higher than expected due to a crud burst during shutdown
required. Twenty-eight workers were whole body counted, with 26 showing uptakes of
  and the temporary loss of RWCS allowed Co-60 to enter and remain in the coolant,
varying levels of Co-60, Co-58, and Mn-54.
  possibly plating out on reactor internals. The second condition related to the
There were three conditions that contributed to the cause of the event. First of all,
  temperature of the material vented from the reactor vessel head. Reactor vessel
coolant activity levels were higher than expected due to a crud burst during shutdown
  outside shell temperatures indicated 215 degrees F, which equates to internal metal
and the temporary loss of RWCS allowed Co-60 to enter and remain in the coolant,
  temperatures above the atmospheric boiling point of water. This indicates that some of
possibly plating out on reactor internals. The second condition related to the
  the coolant flashed to steam as the level in the reactor vessel rose, which could increase
temperature of the material vented from the reactor vessel head. Reactor vessel
  the carryover of coolant activity to the vented gas. The third condition was the
outside shell temperatures indicated 215 degrees F, which equates to internal metal
  inadequate processing of vented material from the reactor vessel head. The venting of
temperatures above the atmospheric boiling point of water. This indicates that some of
  the airborne radioactive particulate would not have resulted in building contamination
the coolant flashed to steam as the level in the reactor vessel rose, which could increase
  and personnel uptakes if the ventilation unit had effectively removed this material to the
the carryover of coolant activity to the vented gas. The third condition was the
  SGTS.
inadequate processing of vented material from the reactor vessel head. The venting of
  The use of the ventilation system was not in accordance with its design configuration.
the airborne radioactive particulate would not have resulted in building contamination
  The ventilation system for previous outages had suction hoses connected to a hood that
and personnel uptakes if the ventilation unit had effectively removed this material to the
  was placed over the reactor vessel head vent, to improve the capture of vented material.
SGTS.
  The use of the hood was discontinued due to its impact on water level instrumentation.
The use of the ventilation system was not in accordance with its design configuration.  
                                            22                                      Enclosure
The ventilation system for previous outages had suction hoses connected to a hood that
was placed over the reactor vessel head vent, to improve the capture of vented material.  
The use of the hood was discontinued due to its impact on water level instrumentation.  


Enclosure
23
An engineering evaluation was not performed on the impact of the change in
An engineering evaluation was not performed on the impact of the change in
configuration of the ventilation system. In addition, the exhaust arrangement from the
configuration of the ventilation system. In addition, the exhaust arrangement from the
ventilation unit to the SGTS had not been evaluated for effectiveness. Licensee
ventilation unit to the SGTS had not been evaluated for effectiveness. Licensee
Procedure MES12, Performing Temporary Modifications, requires the modification
Procedure MES12, Performing Temporary Modifications, requires the modification
process be followed and an evaluation be performed.
process be followed and an evaluation be performed.
Furthermore, licensee procedural guidance did not exist for the overall process of taking
Furthermore, licensee procedural guidance did not exist for the overall process of taking
the operating reactor to a condition allowing fuel movement. The event could have been
the operating reactor to a condition allowing fuel movement. The event could have been
prevented if appropriate acceptance criteria for allowable reactor vessel temperature
prevented if appropriate acceptance criteria for allowable reactor vessel temperature
and coolant activity levels existed. Thus, the root cause of the event was determined to
and coolant activity levels existed. Thus, the root cause of the event was determined to
be a procedural and programmatic weakness.
be a procedural and programmatic weakness.
The licensee initiated CARD 06-21534, Continuous Air Monitor Alarm on Refueling
The licensee initiated CARD 06-21534, Continuous Air Monitor Alarm on Refueling
Floor, to track the investigation of the event in their CAP. The primary corrective action
Floor, to track the investigation of the event in their CAP. The primary corrective action
recommendation is to develop and implement an acceptable methodology for raising
recommendation is to develop and implement an acceptable methodology for raising
reactor vessel water level. In addition, the design and configuration of the current
reactor vessel water level. In addition, the design and configuration of the current
ventilation exhaust capture system will be evaluated and modified, as appropriate to
ventilation exhaust capture system will be evaluated and modified, as appropriate to
assure that it is adequate for the expected reactor vessel fill rate and radioactive
assure that it is adequate for the expected reactor vessel fill rate and radioactive
material concentrations. The methodology may involve an alternate vent path, such as
material concentrations. The methodology may involve an alternate vent path, such as
using the attached piping to vent the reactor vessel to the drywell.
using the attached piping to vent the reactor vessel to the drywell.  
Analysis: The inspectors determined the licensees lack of control of the Temporary
Analysis: The inspectors determined the licensees lack of control of the Temporary
Modification process constituted a design control issue. The licensees failure to
Modification process constituted a design control issue. The licensees failure to
adequately control the process used to vent airborne radioactive particulate to the refuel
adequately control the process used to vent airborne radioactive particulate to the refuel
floor during reactor vessel floodup represents a performance deficiency as defined in
floor during reactor vessel floodup represents a performance deficiency as defined in
NRC Inspection Manual Chapter 0612, Appendix B, Issue Screening. The issue was
NRC Inspection Manual Chapter 0612, Appendix B, Issue Screening. The issue was
determined to be more than minor because if left uncorrected the issue could become a
determined to be more than minor because if left uncorrected the issue could become a
more significant safety concern if coolant activity levels were higher or if the vessel was
more significant safety concern if coolant activity levels were higher or if the vessel was
flooded quicker.
flooded quicker.
The finding was assessed using NRC Inspection Manual Chapter 0609, Appendix C,
The finding was assessed using NRC Inspection Manual Chapter 0609, Appendix C,
Occupational Radiation Safety Significance Determination Process due to individual
Occupational Radiation Safety Significance Determination Process due to individual
worker unplanned, unintended dose. The finding was determined to be of very low
worker unplanned, unintended dose. The finding was determined to be of very low
safety significance because the inspectors answered, NO, to all four phase 1
safety significance because the inspectors answered, NO, to all four phase 1
screening questions.
screening questions.
Enforcement: Technical Specification 5.4.1.a requires that procedures recommended in
Enforcement: Technical Specification 5.4.1.a requires that procedures recommended in
Regulatory Guide 1.33, Revision 2, Appendix A, February 1978, be established,
Regulatory Guide 1.33, Revision 2, Appendix A, February 1978, be established,
implemented and maintained. Section 4.a of that document, in part requires
implemented and maintained.   Section 4.a of that document, in part requires
instructions for filling, venting, and draining the reactor pressure vessel. Contrary to the
instructions for filling, venting, and draining the reactor pressure vessel. Contrary to the
above, the initial installation of the ventilation system and the changes made to the
above, the initial installation of the ventilation system and the changes made to the
ventilation system that was used as part of the reactor vessel floodup during outages
ventilation system that was used as part of the reactor vessel floodup during outages
was not processed through the Temporary Modification Procedure. This finding is being
was not processed through the Temporary Modification Procedure. This finding is being
treated as an NCV, consistent with Section VI.A.1 of the NRC Enforcement Policy and is
treated as an NCV, consistent with Section VI.A.1 of the NRC Enforcement Policy and is
identified as NCV 05000341/2006003-06: Inadequate Controls for Venting the Reactor
identified as NCV 05000341/2006003-06: Inadequate Controls for Venting the Reactor
Pressure Vessel Head. This issue is in the licensees corrective action program as
Pressure Vessel Head. This issue is in the licensees corrective action program as
CARD 06-22667.
CARD 06-22667.
                                          23                                    Enclosure


.2 Forced Outage 06-01
Enclosure
a. Inspection Scope
24
    The inspectors observed the licensees performance during Forced Outage 06-01 from
.2
    May 20, 2006, through May 29, 2006, which was scheduled to locate and replace a
Forced Outage 06-01
    failed fuel assembly. During power ascension following RF11, operators identified a
  a.
    potential fuel leak because off gas radiation levels were slightly elevated from normal.
Inspection Scope
    Operators began suppression testing later that day, which identified the failed assembly.
The inspectors observed the licensees performance during Forced Outage 06-01 from
    Operators initiated a manual unit shutdown to replace the failed fuel. While the unit was
May 20, 2006, through May 29, 2006, which was scheduled to locate and replace a
    shutdown, additional assemblies subjected to similar flux profile histories were also
failed fuel assembly. During power ascension following RF11, operators identified a
    replaced although fuel sipping operations identified only one fuel assembly with a fuel
potential fuel leak because off gas radiation levels were slightly elevated from normal.  
    cladding defect.
Operators began suppression testing later that day, which identified the failed assembly.  
    This inspection consisted of a review of the licensees outage schedule, safe shutdown
Operators initiated a manual unit shutdown to replace the failed fuel. While the unit was
    plan and administrative procedures governing the outage, periodic observations of
shutdown, additional assemblies subjected to similar flux profile histories were also
    equipment alignment, and plant and control room outage activities. Specifically, the
replaced although fuel sipping operations identified only one fuel assembly with a fuel
    inspectors determined whether the licensee effectively managed elements of shutdown
cladding defect.
    risk pertaining to reactivity control, decay heat removal, inventory control, electrical
This inspection consisted of a review of the licensees outage schedule, safe shutdown
    power control, and containment integrity.
plan and administrative procedures governing the outage, periodic observations of
    The inspectors performed the same daily activities, during the outage as described in
equipment alignment, and plant and control room outage activities. Specifically, the
    Section 1R20.1 for the refueling outage.
inspectors determined whether the licensee effectively managed elements of shutdown
    These activities represented one forced outage inspection sample.
risk pertaining to reactivity control, decay heat removal, inventory control, electrical
b. Findings
power control, and containment integrity.  
    No findings of significance were identified.
The inspectors performed the same daily activities, during the outage as described in
.3 Forced Outage 06-02
Section 1R20.1 for the refueling outage.
a. Inspection Scope
These activities represented one forced outage inspection sample.
    The inspectors observed the licensees performance during Forced Outage 06-02 from
  b.
    June 15, 2006, through June 17, 2006. On June 15, a reactor scram occurred due to a
Findings
    main turbine generator trip which occurred when main unit transformer 2B failed. The
No findings of significance were identified.
    inspectors responded to the control room and to the transformer area to assess the
.3
    licensees response to the event.
Forced Outage 06-02
    This inspection consisted of a review of the licensees outage schedule, safe shutdown
 
    plan and administrative procedures governing the outage, and plant and control room
  a.
    outage activities. Specifically, the inspectors determined whether the licensee
Inspection Scope
    effectively managed elements of shutdown risk pertaining to reactivity control, decay
The inspectors observed the licensees performance during Forced Outage 06-02 from
    heat removal, inventory control, and electrical power control.
June 15, 2006, through June 17, 2006. On June 15, a reactor scram occurred due to a
                                              24                                      Enclosure
main turbine generator trip which occurred when main unit transformer 2B failed. The
inspectors responded to the control room and to the transformer area to assess the
licensees response to the event.
This inspection consisted of a review of the licensees outage schedule, safe shutdown
plan and administrative procedures governing the outage, and plant and control room
outage activities. Specifically, the inspectors determined whether the licensee
effectively managed elements of shutdown risk pertaining to reactivity control, decay
heat removal, inventory control, and electrical power control.  


    The inspectors performed the following activities during the outage:
Enclosure
    *       attended control room operator and outage management turnover meetings to
25
            verify the current shutdown risk status was well understood and communicated;
The inspectors performed the following activities during the outage:
    *       performed walkdowns of the main control room to observe the alignment of
*
            systems important to shutdown risk;
attended control room operator and outage management turnover meetings to
    *       observed the operability of RCS instrumentation and compared channels and
verify the current shutdown risk status was well understood and communicated;
            trains against one another; and
*
    *       observed control rod withdrawal to criticality and portions of the plant power
performed walkdowns of the main control room to observe the alignment of  
            ascension.
systems important to shutdown risk;
    These activities represented one forced outage inspection sample.
*
b. Findings
observed the operability of RCS instrumentation and compared channels and
    No findings of significance were identified.
trains against one another; and  
1R22 Surveillance Testing (71111.22Q)
*
a. Inspection Scope
observed control rod withdrawal to criticality and portions of the plant power
    The inspectors reviewed the test results for the following activities to determine whether
ascension.
    risk-significant systems and equipment were capable of performing their intended safety
These activities represented one forced outage inspection sample.
    function and to verify testing was conducted in accordance with applicable procedural
  b.
    and TS requirements:
Findings
    *       MSIV Limit Switch (routine);
No findings of significance were identified.
    *       SLC Squib Valve Test (routine);
1R22
    *       Integrity Test for Containment Penetrations X-7A, X-7B, X-7C, and X-7D (LLRT);
Surveillance Testing (71111.22Q)
    *       Scram Nitrogen Accumulator Integrity Test (routine);
  a.
    *       Scram Discharge Volume Vent and Drain Valves Operability (routine);
Inspection Scope
    *       Secondary Containment Integrity Test (LLRT);
The inspectors reviewed the test results for the following activities to determine whether
    *       MSIV Channel Functional Test (isolation valve);
risk-significant systems and equipment were capable of performing their intended safety
    *       LOOP/LOCA Test (routine);
function and to verify testing was conducted in accordance with applicable procedural
    *       Reactor Core Isolation Cooling System Automatic Actuation and Flow Test
and TS requirements:
            (routine); and
*
    *       High Pressure Coolant Injection Flow Rate Test at 165 psig Reactor Steam
MSIV Limit Switch (routine);
            Pressure (routine).
*
    The inspectors reviewed the test methodology and test results to verify equipment
SLC Squib Valve Test (routine);
    performance was consistent with safety analysis and design basis assumptions. In
*
    addition, the inspectors verified surveillance testing problems were being entered into
Integrity Test for Containment Penetrations X-7A, X-7B, X-7C, and X-7D (LLRT);
    the corrective action program with the appropriate significance characterization.
*
    These activities represented seven routine, two local leak rate test (LLRT), and one
Scram Nitrogen Accumulator Integrity Test (routine);
    containment isolation valve surveillance inspection samples.
*
                                              25                                      Enclosure
Scram Discharge Volume Vent and Drain Valves Operability (routine);
*
Secondary Containment Integrity Test (LLRT);
*
MSIV Channel Functional Test (isolation valve);
*
LOOP/LOCA Test (routine);
*
Reactor Core Isolation Cooling System Automatic Actuation and Flow Test
(routine); and  
*
High Pressure Coolant Injection Flow Rate Test at 165 psig Reactor Steam
Pressure (routine).
The inspectors reviewed the test methodology and test results to verify equipment
performance was consistent with safety analysis and design basis assumptions. In
addition, the inspectors verified surveillance testing problems were being entered into
the corrective action program with the appropriate significance characterization.
These activities represented seven routine, two local leak rate test (LLRT), and one
containment isolation valve surveillance inspection samples.


   b. Findings
Enclosure
    No findings of significance were identified.
26
   b.
Findings
No findings of significance were identified.
1EP6 Drill Evaluation (71114.06)
1EP6 Drill Evaluation (71114.06)
   a. Inspection Scope
   a.
    The inspectors observed the licensee perform classifications and protective action
Inspection Scope
    recommendations during licensed operator requalification training on June 20, 2006.
The inspectors observed the licensee perform classifications and protective action
    The inspectors observed activities in the control room simulator. The inspectors also
recommendations during licensed operator requalification training on June 20, 2006.
    attended the post-drill critique in the simulator. The focus of the inspectors activities
The inspectors observed activities in the control room simulator. The inspectors also
    was to note any weaknesses and deficiencies in the shift managers performance as
attended the post-drill critique in the simulator. The focus of the inspectors activities
    emergency director and ensure the licensee evaluators noted the same weaknesses
was to note any weaknesses and deficiencies in the shift managers performance as
    and deficiencies and entered them into the corrective action program. As part of the
emergency director and ensure the licensee evaluators noted the same weaknesses
    inspection, the inspectors reviewed the drill package included in the list of documents
and deficiencies and entered them into the corrective action program. As part of the
    reviewed at the end of this report.
inspection, the inspectors reviewed the drill package included in the list of documents
    These activities represented one drill evaluation inspection sample.
reviewed at the end of this report.
   b. Findings
These activities represented one drill evaluation inspection sample.
    No findings of significance were identified.
   b.
Findings
No findings of significance were identified.
2OS1 Access Control to Radiologically Significant Areas (IP 71121.01)
2OS1 Access Control to Radiologically Significant Areas (IP 71121.01)
.1   Plant Walkdowns and Radiation Work Permit Reviews
.1
   a. Inspection Scope
Plant Walkdowns and Radiation Work Permit Reviews
    The inspectors reviewed licensee controls and surveys in the following three
   a.
    radiologically significant work areas within radiation areas, high radiation areas and
Inspection Scope
    airborne radioactivity areas in the plant and reviewed work packages which included
The inspectors reviewed licensee controls and surveys in the following three
    associated licensee controls and surveys of these areas to determine if radiological
radiologically significant work areas within radiation areas, high radiation areas and
    controls including surveys, postings and barricades were acceptable:
airborne radioactivity areas in the plant and reviewed work packages which included
    *   Turbine Building Main Steam Reheater Replacement;
associated licensee controls and surveys of these areas to determine if radiological
    *   Drywell Activities; and
controls including surveys, postings and barricades were acceptable:  
    *   Refuel Floor Activities.
*
    These activities represented one inspection sample.
Turbine Building Main Steam Reheater Replacement;
    The inspectors reviewed the radiation work permits (RWPs) and work packages used to
*
    access the three areas and other high radiation work areas to identify the work control
Drywell Activities; and
    instructions and control barriers that had been specified. Electronic dosimeter alarm set
*
    points for both integrated dose and dose rate were evaluated for conformity with survey
Refuel Floor Activities.  
    indications and plant policy. Workers were interviewed to verify they were aware of the
These activities represented one inspection sample.
    actions required when their electronic dosimeters noticeably malfunctioned or alarmed.
The inspectors reviewed the radiation work permits (RWPs) and work packages used to
                                              26                                    Enclosure
access the three areas and other high radiation work areas to identify the work control
instructions and control barriers that had been specified. Electronic dosimeter alarm set
points for both integrated dose and dose rate were evaluated for conformity with survey
indications and plant policy. Workers were interviewed to verify they were aware of the
actions required when their electronic dosimeters noticeably malfunctioned or alarmed.


    These activities represented one inspection sample.
Enclosure
    The inspectors walked down and surveyed (using an NRC survey meter) the three areas
27
    to verify the prescribed RWPs, procedure, and engineering controls were in place,
These activities represented one inspection sample.
    licensee surveys and postings were complete and accurate, and air samplers were
The inspectors walked down and surveyed (using an NRC survey meter) the three areas
    properly located.
to verify the prescribed RWPs, procedure, and engineering controls were in place,
    These activities represented one inspection sample.
licensee surveys and postings were complete and accurate, and air samplers were
    The inspectors reviewed RWPs for the following airborne radioactivity areas to verify
properly located.
    barrier integrity and engineering controls performance, e.g., high efficiency particulate
These activities represented one inspection sample.
    air filter ventilation system operation, and to determine if there was a potential for
The inspectors reviewed RWPs for the following airborne radioactivity areas to verify
    individual worker internal exposures of greater than 50 millirem committed effective
barrier integrity and engineering controls performance, e.g., high efficiency particulate
    dose equivalent. There were no areas where there was a potential for individual worker
air filter ventilation system operation, and to determine if there was a potential for
    internal exposures of greater than 50 millirem committed effective dose equivalent.
individual worker internal exposures of greater than 50 millirem committed effective
    Work areas having a history of, or the potential for, airborne transuranic isotopes were
dose equivalent. There were no areas where there was a potential for individual worker
    evaluated to verify the licensee had considered the potential for transuranic isotopes
internal exposures of greater than 50 millirem committed effective dose equivalent.  
    and provided appropriate worker protection. There where no areas having a history of,
Work areas having a history of, or the potential for, airborne transuranic isotopes were
    or the potential for, airborne transuranic isotopes.
evaluated to verify the licensee had considered the potential for transuranic isotopes
    These activities represented one inspection sample.
and provided appropriate worker protection. There where no areas having a history of,
    The adequacy of the licensees internal dose assessment process for any actual internal
or the potential for, airborne transuranic isotopes.
    exposures greater than 50 millirem committed effective dose equivalent was assessed.
These activities represented one inspection sample.
    There were no internal exposures greater than 50 millirem committed effective dose
The adequacy of the licensees internal dose assessment process for any actual internal
    equivalent.
exposures greater than 50 millirem committed effective dose equivalent was assessed.  
    These activities represented one inspection sample.
There were no internal exposures greater than 50 millirem committed effective dose
   b. Findings
equivalent.
    No findings of significance were identified.
These activities represented one inspection sample.
.2   Problem Identification and Resolution
   b.
   a. Inspection Scope
Findings
    The inspectors reviewed three corrective action reports related to access controls and
No findings of significance were identified.
    high radiation area radiological incidents. Staff members were interviewed and
.2
    corrective action documents were reviewed to verify that follow-up activities were being
Problem Identification and Resolution
    conducted in an effective and timely manner commensurate with their importance to
   a.
    safety and risk based on the following:
Inspection Scope
    *   initial problem identification, characterization, and tracking;
The inspectors reviewed three corrective action reports related to access controls and
    *   disposition of operability/reportability issues;
high radiation area radiological incidents. Staff members were interviewed and
    *   evaluation of safety significance/risk and priority for resolution;
corrective action documents were reviewed to verify that follow-up activities were being
    *   identification of repetitive problems;
conducted in an effective and timely manner commensurate with their importance to
    *   identification of contributing causes;
safety and risk based on the following:
    *   identification and implementation of effective corrective actions;
*
                                                27                                    Enclosure
initial problem identification, characterization, and tracking;
*
disposition of operability/reportability issues;
*
evaluation of safety significance/risk and priority for resolution;
*
identification of repetitive problems;  
*
identification of contributing causes;
*
identification and implementation of effective corrective actions;


    *   resolution of NCVs tracked in the corrective action system; and
Enclosure
    *   implementation/consideration of risk-significant operational experience feedback.
28
    These activities represented one inspection sample.
*
   b. Findings
resolution of NCVs tracked in the corrective action system; and
    No findings of significance were identified.
*
.3   Job-In-Progress Reviews
implementation/consideration of risk-significant operational experience feedback.
   a. Inspection Scope
These activities represented one inspection sample.
    The inspectors observed the following three jobs that were being performed in radiation
   b.
    areas, airborne radioactivity areas, or high radiation areas for observation of work
Findings
    activities that presented the greatest radiological risk to workers:
No findings of significance were identified.  
    *   Drywell Cooler Number Four Removal;
.3
    *   Cutout and Replace Check Valve E1100F031A; and
Job-In-Progress Reviews
    *   Perform Refuel Activities.
   a.
    The inspectors reviewed radiological job requirements for the three activities including
Inspection Scope
    RWP requirements and work procedure requirements, and attended As-Low-As-Is-
The inspectors observed the following three jobs that were being performed in radiation
    Reasonably-Achievable (ALARA) job briefings.
areas, airborne radioactivity areas, or high radiation areas for observation of work
    These activities represented one inspection sample.
activities that presented the greatest radiological risk to workers:  
    Job performance was observed with respect to these requirements to verify radiological
*
    conditions in the work area were adequately communicated to workers through pre-job
Drywell Cooler Number Four Removal;
    briefings and postings. The inspectors also verified the adequacy of radiological
*
    controls including required radiation, contamination, and airborne surveys for system
Cutout and Replace Check Valve E1100F031A; and
    breaches; radiation protection job coverage which included audio and visual surveillance
*
    for remote job coverage; and contamination controls.
Perform Refuel Activities.
    These activities represented one inspection sample.
The inspectors reviewed radiological job requirements for the three activities including
   b. Findings
RWP requirements and work procedure requirements, and attended As-Low-As-Is-
    No findings of significance were identified.
Reasonably-Achievable (ALARA) job briefings.
.4   Radiation Worker Performance
These activities represented one inspection sample.  
   a. Inspection Scope
Job performance was observed with respect to these requirements to verify radiological
    During job performance observations, the inspectors evaluated radiation worker
conditions in the work area were adequately communicated to workers through pre-job
    performance with respect to stated radiation protection work requirements and
briefings and postings. The inspectors also verified the adequacy of radiological
    evaluated whether workers were aware of the significant radiological conditions in their
controls including required radiation, contamination, and airborne surveys for system
    workplace, the RWP controls and limits in place, and that their performance had
breaches; radiation protection job coverage which included audio and visual surveillance
    accounted for the level of radiological hazards present.
for remote job coverage; and contamination controls.
                                              28                                      Enclosure
These activities represented one inspection sample.
   b.
Findings
No findings of significance were identified.  
.4
Radiation Worker Performance
   a.
Inspection Scope
During job performance observations, the inspectors evaluated radiation worker
performance with respect to stated radiation protection work requirements and
evaluated whether workers were aware of the significant radiological conditions in their
workplace, the RWP controls and limits in place, and that their performance had
accounted for the level of radiological hazards present.


    These activities represented one inspection sample.
Enclosure
    The inspectors reviewed radiological problem reports which found the cause of the
29
    event was due to radiation worker errors to determine if there was an observable pattern
These activities represented one inspection sample.
    traceable to a similar cause, and to determine if this perspective matched the corrective
The inspectors reviewed radiological problem reports which found the cause of the
    action approach taken by the licensee to resolve the reported problems. These
event was due to radiation worker errors to determine if there was an observable pattern
    problems, along with planned and taken corrective actions were discussed with the
traceable to a similar cause, and to determine if this perspective matched the corrective
    Radiation Protection Manager.
action approach taken by the licensee to resolve the reported problems. These
    These activities represented one inspection sample.
problems, along with planned and taken corrective actions were discussed with the
   b. Findings
Radiation Protection Manager.
    No findings of significance were identified.
These activities represented one inspection sample.
.5   Radiation Protection Technician (RPT) Proficiency
   b.
   a. Inspection Scope
Findings
    During job performance observations, the inspectors evaluated RPT performance with
No findings of significance were identified.
    respect to radiation protection work requirements and evaluated whether they were
.5
    aware of the radiological conditions in their workplace, the RWP controls and limits in
Radiation Protection Technician (RPT) Proficiency
    place, and if their performance was consistent with their training and qualifications with
   a.
    respect to the radiological hazards and work activities.
Inspection Scope
    These activities represented one inspection sample.
During job performance observations, the inspectors evaluated RPT performance with
    The inspectors reviewed two radiological problem reports which found the cause of the
respect to radiation protection work requirements and evaluated whether they were
    event was radiation protection technician error to determine if there was an observable
aware of the radiological conditions in their workplace, the RWP controls and limits in
    pattern traceable to a similar cause, and to determine if this perspective matched the
place, and if their performance was consistent with their training and qualifications with
    corrective action approach taken by the licensee to resolve the reported problems.
respect to the radiological hazards and work activities.
    These activities represented one inspection sample.
These activities represented one inspection sample.
   b. Findings
The inspectors reviewed two radiological problem reports which found the cause of the
    No findings of significance were identified.
event was radiation protection technician error to determine if there was an observable
pattern traceable to a similar cause, and to determine if this perspective matched the
corrective action approach taken by the licensee to resolve the reported problems.
These activities represented one inspection sample.
   b.
Findings
No findings of significance were identified.
2OS2 As-Low-As-Is-Reasonably-Achievable Planning And Controls (ALARA) (IP 71121.02)
2OS2 As-Low-As-Is-Reasonably-Achievable Planning And Controls (ALARA) (IP 71121.02)
.1   Inspection Planning
.1
   a. Inspection Scope
Inspection Planning
    The inspectors reviewed plant collective exposure history, current exposure trends,
   a.
    ongoing and planned activities in order to assess current performance and exposure
Inspection Scope
    challenges. This included determining the plants current 3-year rolling average for
The inspectors reviewed plant collective exposure history, current exposure trends,  
    collective exposure in order to help establish resource allocations and to provide a
ongoing and planned activities in order to assess current performance and exposure
    perspective of significance for any resulting inspection finding assessment.
challenges. This included determining the plants current 3-year rolling average for
                                              29                                      Enclosure
collective exposure in order to help establish resource allocations and to provide a
perspective of significance for any resulting inspection finding assessment.


    These activities represented one inspection sample.
Enclosure
    The inspectors reviewed the outage work scheduled during the inspection period and
30
    associated work activity exposure estimates for the following five work activities which
These activities represented one inspection sample.
    were likely to result in the highest personnel collective exposures:
The inspectors reviewed the outage work scheduled during the inspection period and
    *   Drywell Cooler Number Four Removal;
associated work activity exposure estimates for the following five work activities which
    *   Cutout and Replace Check Valve E1100F031A;
were likely to result in the highest personnel collective exposures:  
    *   Refuel Floor Activities;
*
    *   Main Steam Reheater Replacement; and
Drywell Cooler Number Four Removal;
    *   In-Service Inspections.
*
    These activities represented one inspection sample.
Cutout and Replace Check Valve E1100F031A;
    The inspectors determined site specific trends in collective exposures and source-term
*
    measurements. The inspectors reviewed procedures associated with maintaining
Refuel Floor Activities;
    occupational exposures ALARA and processes used to estimate and track work activity
*
    specific exposures.
Main Steam Reheater Replacement; and
    These activities represented two inspection samples.
*
   b. Findings
In-Service Inspections.
    No findings of significance were identified.
These activities represented one inspection sample.
.2   Radiological Work Planning
The inspectors determined site specific trends in collective exposures and source-term
   a. Inspection Scope
measurements. The inspectors reviewed procedures associated with maintaining
    The inspectors evaluated the licensees list of planned work activities for RF11 ranked
occupational exposures ALARA and processes used to estimate and track work activity
    by estimated exposure that were in progress and reviewed the following three work
specific exposures.
    activities of exposure significance:
These activities represented two inspection samples.
    *   06-1113, CRD Exchange;
   b.
    *   06-1205, East/West MSR Replacement; and
Findings
    *   06-1124, Drywell Cooler Number Four Removal.
No findings of significance were identified.
    For these three activities, the inspectors reviewed the ALARA work activity evaluations,
.2
    exposure estimates, and exposure mitigation requirements in order to verify the licensee
Radiological Work Planning
    had established procedures and engineering and work controls that were based on
   a.
    sound radiation protection principles in order to achieve occupational exposures that
Inspection Scope
    were ALARA. This also involved determining that the licensee had reasonably grouped
The inspectors evaluated the licensees list of planned work activities for RF11 ranked
    the radiological work into work activities, based on historical precedence, industry
by estimated exposure that were in progress and reviewed the following three work
    norms, and/or special circumstances.
activities of exposure significance:  
    The inspectors compared the results achieved including dose rate reductions and
*
    person-rem used with the intended dose established in the licensees ALARA planning
06-1113, CRD Exchange;
    for these three work activities. Reasons for inconsistencies between intended and
*
    actual work activity doses were reviewed.
06-1205, East/West MSR Replacement; and
                                              30                                    Enclosure
*
06-1124, Drywell Cooler Number Four Removal.
For these three activities, the inspectors reviewed the ALARA work activity evaluations,
exposure estimates, and exposure mitigation requirements in order to verify the licensee
had established procedures and engineering and work controls that were based on
sound radiation protection principles in order to achieve occupational exposures that
were ALARA. This also involved determining that the licensee had reasonably grouped
the radiological work into work activities, based on historical precedence, industry
norms, and/or special circumstances.
The inspectors compared the results achieved including dose rate reductions and
person-rem used with the intended dose established in the licensees ALARA planning
for these three work activities. Reasons for inconsistencies between intended and
actual work activity doses were reviewed.


      These activities represented one inspection sample.
Enclosure
   b. Findings
31
      No findings of significance were identified.
These activities represented one inspection sample.
.3   Verification of Dose Estimates and Exposure Tracking Systems
   b.
   a. Inspection Scope
Findings
      The licensees process for adjusting exposure estimates or re-planning work, when
No findings of significance were identified.
      unexpected changes in scope, emergent work or higher than anticipated radiation levels
.3
      were encountered, was evaluated. This included determining that adjustments to
Verification of Dose Estimates and Exposure Tracking Systems
      estimated exposure (intended dose) were based on sound radiation protection and
   a.
      ALARA principles and not adjusted to account for failures to control the work. The
Inspection Scope
      frequency of these adjustments was reviewed to evaluate the adequacy of the original
The licensees process for adjusting exposure estimates or re-planning work, when
      ALARA planning process.
unexpected changes in scope, emergent work or higher than anticipated radiation levels
      These activities represented one inspection sample.
were encountered, was evaluated. This included determining that adjustments to
   b. Findings
estimated exposure (intended dose) were based on sound radiation protection and
      No findings of significance were identified.
ALARA principles and not adjusted to account for failures to control the work. The
.4   Job Site Inspections and ALARA Control
frequency of these adjustments was reviewed to evaluate the adequacy of the original
   a. Inspection Scope
ALARA planning process.
      The inspectors observed the following five jobs that were being performed in radiation
These activities represented one inspection sample.
      areas, airborne radioactivity areas, or high radiation areas for observation of work
   b.
      activities that presented the greatest radiological risk to workers.
Findings
      *   Drywell Cooler Number Four Removal;
No findings of significance were identified.
      *   Cutout and Replace Check Valve E1100F031A;
.4
      *   Refuel Floor Activities;
Job Site Inspections and ALARA Control
      *   Main Steam Reheater Replacement; and
   a.
      *   In-Service Inspections.
Inspection Scope
      The licensees use of engineering controls to achieve dose reductions was evaluated to
The inspectors observed the following five jobs that were being performed in radiation
      verify procedures and controls were consistent with the licensees ALARA reviews,
areas, airborne radioactivity areas, or high radiation areas for observation of work
      sufficient shielding of radiation sources was provided for, and the dose expended to
activities that presented the greatest radiological risk to workers.
      install/remove the shielding did not exceed the dose reduction benefits afforded by the
*
      shielding.
Drywell Cooler Number Four Removal;
      These activities represented one inspection sample.
*
   b. Findings
Cutout and Replace Check Valve E1100F031A;
      No findings of significance were identified.
*
                                              31                                      Enclosure
Refuel Floor Activities;
*
Main Steam Reheater Replacement; and
*
In-Service Inspections.
The licensees use of engineering controls to achieve dose reductions was evaluated to
verify procedures and controls were consistent with the licensees ALARA reviews,
sufficient shielding of radiation sources was provided for, and the dose expended to
install/remove the shielding did not exceed the dose reduction benefits afforded by the
shielding.
These activities represented one inspection sample.
   b.
Findings
No findings of significance were identified.  


.5   Radiation Worker Performance
Enclosure
   a. Inspection Scope
32
      Radiation worker and RPT performance was observed during work activities being
.5
      performed in radiation areas, airborne radioactivity areas, and high radiation areas that
Radiation Worker Performance
      presented the greatest radiological risk to workers. The inspectors evaluated whether
   a.
      workers demonstrated the ALARA philosophy in practice by being familiar with the work
Inspection Scope
      activity scope and tools to be used, by utilizing ALARA low dose waiting areas, and that
Radiation worker and RPT performance was observed during work activities being
      work activity controls were being complied with. Also, radiation worker training and skill
performed in radiation areas, airborne radioactivity areas, and high radiation areas that
      levels were reviewed to determine if they were sufficient relative to the radiological
presented the greatest radiological risk to workers. The inspectors evaluated whether
      hazards and the work involved.
workers demonstrated the ALARA philosophy in practice by being familiar with the work
      These activities represented one inspection sample.
activity scope and tools to be used, by utilizing ALARA low dose waiting areas, and that
   b. Findings
work activity controls were being complied with. Also, radiation worker training and skill
      No findings of significance were identified.
levels were reviewed to determine if they were sufficient relative to the radiological
4.   OTHER ACTIVITIES (OA)
hazards and the work involved.
These activities represented one inspection sample.
   b.
Findings
No findings of significance were identified.
4.
OTHER ACTIVITIES (OA)
  4OA2 Identification and Resolution of Problems (71152)
  4OA2 Identification and Resolution of Problems (71152)
  .1   Routine Review of Identification and Resolution of Problems
  .1
   a.  Inspection Scope
Routine Review of Identification and Resolution of Problems
      As discussed in previous sections of this report, the inspectors routinely reviewed issues
   a.   
      during baseline inspection activities and plant status reviews to verify they were being
Inspection Scope
      entered into the licensee's corrective action system at an appropriate threshold,
As discussed in previous sections of this report, the inspectors routinely reviewed issues
      adequate attention was being given to timely corrective actions, and adverse trends
during baseline inspection activities and plant status reviews to verify they were being
      were identified and addressed.
entered into the licensee's corrective action system at an appropriate threshold,
   b.  Findings
adequate attention was being given to timely corrective actions, and adverse trends
      No findings of significance were identified.
were identified and addressed.  
  .2  Semi-Annual Trend Review
   b.   
   a. Inspection Scope
Findings
      The inspectors performed a screening review of each item entered into the licensees
No findings of significance were identified.
      corrective action program to identify trends that might indicate the existence of a more
  .2   
      significant safety issue. The inspectors considered repetitive or closely related issues
Semi-Annual Trend Review
      that may have been documented by the licensee outside the normal corrective action
   a.
      program, such as in:
Inspection Scope
      C   trend reports or performance indicators,
The inspectors performed a screening review of each item entered into the licensees
      C   major equipment problem lists,
corrective action program to identify trends that might indicate the existence of a more
                                              32                                      Enclosure
significant safety issue. The inspectors considered repetitive or closely related issues
that may have been documented by the licensee outside the normal corrective action
program, such as in:
C
trend reports or performance indicators,  
C
major equipment problem lists,  


      C   repetitive and/or rework maintenance lists,
Enclosure
      C   departmental problem/challenges lists,
33
      C   system health reports,
C
      C   quality assurance audit/surveillance reports,
repetitive and/or rework maintenance lists,  
      C   self assessment reports,
C
      C   maintenance rule assessments, or
departmental problem/challenges lists,  
      C   corrective action backlog lists.
C
      The inspectors verified the licensee was identifying issues at an appropriate threshold
system health reports,  
      and entering them into their corrective action program by comparing those issues
C
      identified by the NRC during the conduct of the plant status and inspectable area
quality assurance audit/surveillance reports,  
      portions of the program with those issues identified by the licensee.
C
   b. Issues
self assessment reports,  
      Unidentified drywell leakage was fluctuating after startup from RF11 but has since
C
      leveled out. From the lowest value, unidentified leakage has increased from about
maintenance rule assessments, or  
      0.06 gpm to an average daily value of 0.14 gpm. Additionally, the inner seal pressure
C
      for the B reactor recirculation pump has been fluctuating by as much as 40-60 psig;
corrective action backlog lists.
      however, there does not appear to be a correlation between the seal pressure
The inspectors verified the licensee was identifying issues at an appropriate threshold
      oscillations and drywell leakage. These issues are in the licensees corrective action
and entering them into their corrective action program by comparing those issues
      program as CARDs 06-24313 for the unidentified leakage and 06-23791 for the seal
identified by the NRC during the conduct of the plant status and inspectable area
      pressure oscillations.
portions of the program with those issues identified by the licensee.
   b.
Issues
Unidentified drywell leakage was fluctuating after startup from RF11 but has since
leveled out. From the lowest value, unidentified leakage has increased from about
0.06 gpm to an average daily value of 0.14 gpm. Additionally, the inner seal pressure
for the B reactor recirculation pump has been fluctuating by as much as 40-60 psig;
however, there does not appear to be a correlation between the seal pressure
oscillations and drywell leakage. These issues are in the licensees corrective action
program as CARDs 06-24313 for the unidentified leakage and 06-23791 for the seal
pressure oscillations.
4OA3 Event Followup (71153)
4OA3 Event Followup (71153)
.1   Reactor Scram due to Main Transformer Fault
.1
   a. Inspection Scope
Reactor Scram due to Main Transformer Fault
      As described in Section 1R20.3 of this report, the inspectors responded to the control
   a.
      room on June 15, 2006, when the reactor automatically shut down as a result of the
Inspection Scope
      failure of main unit transformer 2B. The inspectors observed plant parameters and
As described in Section 1R20.3 of this report, the inspectors responded to the control
      status, evaluated the performance of mitigating systems and licensee actions, confirmed
room on June 15, 2006, when the reactor automatically shut down as a result of the
      that the licensee properly classified the event in accordance with emergency action level
failure of main unit transformer 2B. The inspectors observed plant parameters and
      procedures and made timely notifications to NRC and state/county governments, as
status, evaluated the performance of mitigating systems and licensee actions, confirmed
      required by 10 CFR 50.72 (Event Number 42643). The inspectors determined and
that the licensee properly classified the event in accordance with emergency action level
      communicated details regarding the event to NRC management, risk analysts and
procedures and made timely notifications to NRC and state/county governments, as
      others in Region III and Headquarters as input to an evaluation per Management
required by 10 CFR 50.72 (Event Number 42643). The inspectors determined and
      Directive 8.3 for determining the appropriate level of event response. Based on the
communicated details regarding the event to NRC management, risk analysts and
      events that occurred, routine resident inspection efforts were deemed appropriate.
others in Region III and Headquarters as input to an evaluation per Management
   b. Findings
Directive 8.3 for determining the appropriate level of event response. Based on the
      No findings of significance were identified.
events that occurred, routine resident inspection efforts were deemed appropriate.
                                              33                                    Enclosure
   b.
Findings
No findings of significance were identified.


.2   Review of Licensee Event Reports (LER)
Enclosure
   a. (Closed) LER 50-341/2006-001: At 0039 hours on April 1, 2006, Fermi 2 feedwater line
34
    check valves B2100F010A and B2100F076A failed their LLRT. The air leakage rate of
.2
    the inboard check valve B2100F010A was 324.21 standard cubic feet per hour (SCFH),
Review of Licensee Event Reports (LER)
    and the leakage rate of outboard check valve B2100F076A was above the
   a.
    measurement capability of the leak rate monitor. The penetration (X-9A) minimum-
(Closed) LER 50-341/2006-001: At 0039 hours on April 1, 2006, Fermi 2 feedwater line
    pathway air leakage value was determined to be 324.21 SCFH which is greater than the
check valves B2100F010A and B2100F076A failed their LLRT. The air leakage rate of
    allowable containment leakage rate (La) value of 296.3 SCFH per TS 5.5.12 and higher
the inboard check valve B2100F010A was 324.21 standard cubic feet per hour (SCFH),
    than the allowable secondary containment bypass leakage rate of 0.1 La or 29.63 SCFH
and the leakage rate of outboard check valve B2100F076A was above the
    per TS Surveillance Requirement 3.6.1.3.11. The B2100F076A failure was attributed to
measurement capability of the leak rate monitor. The penetration (X-9A) minimum-
    soft seat degradation which was primarily caused by extending its service time to three
pathway air leakage value was determined to be 324.21 SCFH which is greater than the
    operating cycles. The B2100F010A valve failure was attributed to soft seat degradation
allowable containment leakage rate (La) value of 296.3 SCFH per TS 5.5.12 and higher
    due to a slight misalignment of the valve disc to the in-body seat, compounded by wear
than the allowable secondary containment bypass leakage rate of 0.1 La or 29.63 SCFH
    between the internal shaft and valve disc. The slight misalignment caused the soft seat
per TS Surveillance Requirement 3.6.1.3.11. The B2100F076A failure was attributed to
    along the top portion of the disc to contact the seat first, resulting in a scraping action as
soft seat degradation which was primarily caused by extending its service time to three
    the disc flexed to its full seat position. For both valves, the soft seats were replaced,
operating cycles. The B2100F010A valve failure was attributed to soft seat degradation
    and the soft seat service time has been limited to two operating cycles. The internal
due to a slight misalignment of the valve disc to the in-body seat, compounded by wear
    shaft for the B2100F010A valve was replaced, and the alignment between the disc and
between the internal shaft and valve disc. The slight misalignment caused the soft seat
    the valve seat was adjusted. Both valves were retested and met their associated LLRT
along the top portion of the disc to contact the seat first, resulting in a scraping action as
    acceptance criteria prior to restart of the unit.
the disc flexed to its full seat position. For both valves, the soft seats were replaced,
    The LER was reviewed by the inspectors. No findings of significance were identified
and the soft seat service time has been limited to two operating cycles. The internal
    and no violation of NRC requirements occurred. The licensee documented the LLRT
shaft for the B2100F010A valve was replaced, and the alignment between the disc and
    failure in CARD 06-21751. This LER is closed.
the valve seat was adjusted. Both valves were retested and met their associated LLRT
acceptance criteria prior to restart of the unit.
The LER was reviewed by the inspectors. No findings of significance were identified
and no violation of NRC requirements occurred. The licensee documented the LLRT
failure in CARD 06-21751. This LER is closed.
4OA6 Exit Meetings
4OA6 Exit Meetings
.1   Exit Meeting Summary
.1
    On July 11, 2006, the inspectors presented the inspection results to Mr. D. Cobb and
Exit Meeting Summary
    other members of licensee management at the conclusion of the inspection. The
On July 11, 2006, the inspectors presented the inspection results to Mr. D. Cobb and
    inspectors asked the licensee whether any material examined during the inspection
other members of licensee management at the conclusion of the inspection. The
    should be considered proprietary. No proprietary information was identified.
inspectors asked the licensee whether any material examined during the inspection
.2   Interim Exit Meetings
should be considered proprietary. No proprietary information was identified.
    On April 7, 2006, an interim exit meeting was conducted for the Access Control to
.2
    Radiological Areas and ALARA inspection with Mr. Kevin Hlavaty, Plant Manager, and
Interim Exit Meetings
    other licensee staff.
On April 7, 2006, an interim exit meeting was conducted for the Access Control to
Radiological Areas and ALARA inspection with Mr. Kevin Hlavaty, Plant Manager, and  
other licensee staff.
4OA7 Licensee-Identified Violations
4OA7 Licensee-Identified Violations
    The following violation of very low significance was identified by the licensee and is a
The following violation of very low significance was identified by the licensee and is a
    violation of NRC requirements, which meet the criteria of Section VI of the NRC
violation of NRC requirements, which meet the criteria of Section VI of the NRC
    Enforcement Manual, NUREG-1600, for being dispositioned as an NCV.
Enforcement Manual, NUREG-1600, for being dispositioned as an NCV.
                                                34                                      Enclosure


    Cornerstone: Public Radiation Safety
Enclosure
    The licensees procedure 67.000.103, Surveying of Outgoing Shipments, directs the
35
    staff to survey outgoing vehicles used to carry an exclusive use shipment of radioactive
Cornerstone: Public Radiation Safety
    material. The procedure relies on the proper identification of the incoming shipment as
The licensees procedure 67.000.103, Surveying of Outgoing Shipments, directs the
    an exclusive use shipment. This procedure is used to implement the requirements of
staff to survey outgoing vehicles used to carry an exclusive use shipment of radioactive
    49 CFR 173.443 and 49 CFR 177.843 that require the specific release survey of
material. The procedure relies on the proper identification of the incoming shipment as
    vehicles in exclusive use situations. Contrary to the above, and as described in
an exclusive use shipment. This procedure is used to implement the requirements of
    CARD 06-21389, on March 20, 2006, an exclusive use radioactive material shipment
49 CFR 173.443 and 49 CFR 177.843 that require the specific release survey of
    was received by the licensee. The shipment contained one package of Limited Quantity
vehicles in exclusive use situations. Contrary to the above, and as described in
    radioactive material and four boxes of non-radioactive material and the radiation
CARD 06-21389, on March 20, 2006, an exclusive use radioactive material shipment
    protection staff assigned to accept the shipment incorrectly identified the shipment as a
was received by the licensee. The shipment contained one package of Limited Quantity
    non-exclusive use shipment. After the packages were removed from the conveyance,
radioactive material and four boxes of non-radioactive material and the radiation
    the vehicle was released without the required survey. This was identified by licensee
protection staff assigned to accept the shipment incorrectly identified the shipment as a
    supervision but not before the vehicle had departed the site. The carrier was contacted
non-exclusive use shipment. After the packages were removed from the conveyance,
    and the vehicle returned to the licensees site before further transportation activity had
the vehicle was released without the required survey. This was identified by licensee
    commenced and a survey was completed. No contamination was found and no dose
supervision but not before the vehicle had departed the site. The carrier was contacted
    rates above background were identified. The finding is of very low safety significance
and the vehicle returned to the licensees site before further transportation activity had
    because it did not result in an unmonitored release nor were any dose limits
commenced and a survey was completed. No contamination was found and no dose
    approached.
rates above background were identified. The finding is of very low safety significance
ATTACHMENT: SUPPLEMENTAL INFORMATION
because it did not result in an unmonitored release nor were any dose limits
                                            35                                      Enclosure
approached.
ATTACHMENT: SUPPLEMENTAL INFORMATION


                                  KEY POINTS OF CONTACT
Attachment
1
KEY POINTS OF CONTACT
Licensee
Licensee
D. Gipson, Chief Nuclear Officer
D. Gipson, Chief Nuclear Officer
Line 1,453: Line 1,759:
NRC
NRC
C. Lipa, Chief, Division of Reactor Projects, Branch 4
C. Lipa, Chief, Division of Reactor Projects, Branch 4
                                                1      Attachment


                LIST OF ITEMS OPENED, CLOSED, AND DISCUSSED
Attachment
2
LIST OF ITEMS OPENED, CLOSED, AND DISCUSSED
Opened
Opened
05000341/2006003-05 URI   Inappropriate Use of Risk in Operability Evaluations
05000341/2006003-05
                            (Section 1R15.3)
URI
Inappropriate Use of Risk in Operability Evaluations
(Section 1R15.3)
Opened and Closed
Opened and Closed
05000341/2006003-01 NCV   Unauthorized Transient Combustibles in Safety-Related
05000341/2006003-01
                            Areas (Section 1R05.2)
NCV
05000341/2006003-02 NCV   Improper Storage of Chemicals Affecting Fire Fighting
Unauthorized Transient Combustibles in Safety-Related
                            Response (Section 1R05.3)
Areas (Section 1R05.2)
05000341/2006003-03 NCV   Inadequate Maintenance Risk Assessment
05000341/2006003-02
                            (Section 1R13.2)
NCV
05000341/2006003-04 NCV   Improper Evaluation of Standby Liquid Control Operability
Improper Storage of Chemicals Affecting Fire Fighting
                            During Tank Sparging (Section 1R15.2)
Response (Section 1R05.3)
05000341/2006003-06 NCV   Inadequate Controls for Venting the Reactor Pressure
05000341/2006003-03
                            Vessel Head (Section 1R20.1)
NCV
Inadequate Maintenance Risk Assessment
(Section 1R13.2)
05000341/2006003-04
NCV
Improper Evaluation of Standby Liquid Control Operability
During Tank Sparging (Section 1R15.2)
05000341/2006003-06
NCV
Inadequate Controls for Venting the Reactor Pressure
Vessel Head (Section 1R20.1)
Closed
Closed
05000341/2006-001   LER   Excessive Feedwater Check Valve Leakage at Containment
05000341/2006-001
                            Penetration
LER
Excessive Feedwater Check Valve Leakage at Containment
Penetration
Discussed
Discussed
None.
None.
                                        2                                    Attachment


                                LIST OF DOCUMENTS REVIEWED
Attachment
The following is a list of documents reviewed during the inspection. Inclusion on this list does
3
LIST OF DOCUMENTS REVIEWED
The following is a list of documents reviewed during the inspection. Inclusion on this list does
not imply that the NRC inspectors reviewed the documents in their entirety but rather that
not imply that the NRC inspectors reviewed the documents in their entirety but rather that
selected sections of portions of the documents were evaluated as part of the overall inspection
selected sections of portions of the documents were evaluated as part of the overall inspection
effort. Inclusion of a document on this list does not imply NRC acceptance of the document or
effort. Inclusion of a document on this list does not imply NRC acceptance of the document or
any part of it, unless this is stated in the body of the inspection report.
any part of it, unless this is stated in the body of the inspection report.
1R01: Adverse Weather Protection
1R01: Adverse Weather Protection
Line 1,493: Line 1,815:
Drawing 6M721-5706-1, 3/5/04; Residual Heat Removal (RHR) Division II Functional Operating
Drawing 6M721-5706-1, 3/5/04; Residual Heat Removal (RHR) Division II Functional Operating
Sketch
Sketch
03-00120, 01/02/03; Pinhole leak in piping
03-00120, 01/02/03; Pinhole leak in piping  
03-13694, 6/17/03; Document the Condition of General Service Water Piping
03-13694, 6/17/03; Document the Condition of General Service Water Piping
04-24918, 10/25/04; P4100F402A installed at the bottom of the pipe
04-24918, 10/25/04; P4100F402A installed at the bottom of the pipe
Line 1,516: Line 1,838:
3/18/06
3/18/06
CARD 06-22600; Moderate Energy Line Break Evaluation; 4/21/06 (NRC-Identified)
CARD 06-22600; Moderate Energy Line Break Evaluation; 4/21/06 (NRC-Identified)
                                                  3                                Attachment


Attachment
4
Nuclear Generation Memo TMPE-94-0308; May 18, 1994; Flood Protection Review
Nuclear Generation Memo TMPE-94-0308; May 18, 1994; Flood Protection Review
6M721-2223, Rev U, 11/24/06; Diagram Equipment Drains All Floors Auxiliary and Reactor
6M721-2223, Rev U, 11/24/06; Diagram Equipment Drains All Floors Auxiliary and Reactor
Line 1,559: Line 1,882:
Fermi 2 Daily Plant Status, April 17, 2006
Fermi 2 Daily Plant Status, April 17, 2006
Schedulers Evaluation for Fermi 2, April 17, 2006
Schedulers Evaluation for Fermi 2, April 17, 2006
                                                4                                Attachment


Attachment
5
Fermi 2 Daily Plant Status, April 30, 2006
Fermi 2 Daily Plant Status, April 30, 2006
Schedulers Evaluation for Fermi 2, April 30, 2006
Schedulers Evaluation for Fermi 2, April 30, 2006
Line 1,594: Line 1,918:
CARD 99-13240; Inoperability of Standby Liquid Control During Air Sparging; 4/15/99
CARD 99-13240; Inoperability of Standby Liquid Control During Air Sparging; 4/15/99
1R19: Post-Maintenance Testing
1R19: Post-Maintenance Testing
EDP - 31880 120 KV Switchyard Upgrade
EDP - 31880 120 KV Switchyard Upgrade  
Engineering Change Request 33690-1, Rev A, 03/14/06; Replacement of Drywell Cooler Coils
Engineering Change Request 33690-1, Rev A, 03/14/06; Replacement of Drywell Cooler Coils
T470B003 and T4700B004
T470B003 and T4700B004
Line 1,604: Line 1,928:
CARD 06-22982, 4/30/06; Inboard MSIV A will not slow close
CARD 06-22982, 4/30/06; Inboard MSIV A will not slow close
CARD 06-23031, 5/1/06; MSIV B2103F028B RPS Limit Switch did not actuate when expected
CARD 06-23031, 5/1/06; MSIV B2103F028B RPS Limit Switch did not actuate when expected
                                                5                                  Attachment


Attachment
6
CARD 06-22634, 4/22/06; A Inboard MSIV limit switch, PIS B21N572A, will not change state
CARD 06-22634, 4/22/06; A Inboard MSIV limit switch, PIS B21N572A, will not change state
Drawing SD-F-0179, Rev. A, 9/25/05; Diagram Line Breaker Control 120KV, POS GK
Drawing SD-F-0179, Rev. A, 9/25/05; Diagram Line Breaker Control 120KV, POS GK
Line 1,625: Line 1,950:
Apparent Cause Determination for Damage Found in the Main Generator During RF11 Robot
Apparent Cause Determination for Damage Found in the Main Generator During RF11 Robot
Inspections CARD 06-21922
Inspections CARD 06-21922
Inspection Requirement Form, Requisition Number: 9086929; 04/19/2006
Inspection Requirement Form, Requisition Number: 9086929; 04/19/2006
Drawing 6M721-3722, Rev A; Flow Diagram & Details of Purging Unit - Reactor Pressure
Drawing 6M721-3722, Rev A; Flow Diagram & Details of Purging Unit - Reactor Pressure
Vessel - Unit 2
Vessel - Unit 2
Line 1,634: Line 1,959:
CARD 06-22642, 04/22/2006; Are EDG Surveillances Testing What They Are Setup to Test
CARD 06-22642, 04/22/2006; Are EDG Surveillances Testing What They Are Setup to Test
CARD 06-22667, 04/23/2006; RPV Venting Unit Configuration Control Discrepancies
CARD 06-22667, 04/23/2006; RPV Venting Unit Configuration Control Discrepancies
CARD 06-23114, 05/03/2006; NRC Concern: Review of ERE-34173 E1150F608 MOV Motor
CARD 06-23114, 05/03/2006; NRC Concern: Review of ERE-34173 E1150F608 MOV Motor
Replacement
Replacement
CARD 06-23793, 06/02/2006; NRC Concern - Material Released Without the Requirements of
CARD 06-23793, 06/02/2006; NRC Concern - Material Released Without the Requirements of
Line 1,649: Line 1,974:
Work Control Conduct Manual MWC13, Rev 0; Outage Nuclear Safety
Work Control Conduct Manual MWC13, Rev 0; Outage Nuclear Safety
Maintenance Conduct Manual MMA07, Rev 14; Hoisting, Rigging and Load Handling
Maintenance Conduct Manual MMA07, Rev 14; Hoisting, Rigging and Load Handling
                                            6                                  Attachment


Attachment
7
1R22: Surveillance Testing
1R22: Surveillance Testing
Drawing 6M721-5703-1, Rev. Y; Control Rod Drive System Functional Operating Sketch
Drawing 6M721-5703-1, Rev. Y; Control Rod Drive System Functional Operating Sketch
Line 1,675: Line 2,001:
Penetration X-7A, X-7B, X-7C, and X-7D
Penetration X-7A, X-7B, X-7C, and X-7D
Procedure 43.401.500, Rev 35; Surveillance Procedure, Local Leakage Rate Testing for
Procedure 43.401.500, Rev 35; Surveillance Procedure, Local Leakage Rate Testing for
Penetration X-7A, X-7B, X-7C, and X-7D
Penetration X-7A, X-7B, X-7C, and X-7D  
Procedure 24.402.06; Rev. 32; Drywell to Suppression Chamber Bypass Leak Test
Procedure 24.402.06; Rev. 32; Drywell to Suppression Chamber Bypass Leak Test
Procedure 35.139.002; Rev. 27; SLC System Explosive Valve Insert Replacement
Procedure 35.139.002; Rev. 27; SLC System Explosive Valve Insert Replacement
Line 1,689: Line 2,015:
Scenario SS-OP-802-3300, Rev. 0; Anticipated Transient Without Scram with Small Steam
Scenario SS-OP-802-3300, Rev. 0; Anticipated Transient Without Scram with Small Steam
Leak; 1/26/06
Leak; 1/26/06
2OS1: Access Control to Radiologically Significant Areas
2OS1: Access Control to Radiologically Significant Areas
CARD 05-26818; Primary Containment Atmosphere Sample Pump; T5001-C003 Will Not Start;
CARD 05-26818; Primary Containment Atmosphere Sample Pump; T5001-C003 Will Not Start;
dated December 5, 2005
dated December 5, 2005
Line 1,695: Line 2,021:
Clothing at Drywell Step-off Pad; dated April 5, 2006
Clothing at Drywell Step-off Pad; dated April 5, 2006
CARD 06-21534; High Radiation Alarm on Refuel Floor; dated March 26, 2006
CARD 06-21534; High Radiation Alarm on Refuel Floor; dated March 26, 2006
                                                7                              Attachment


Attachment
8
CARD 06-21640; Unnecessary Contamination of Personnel; dated March 29, 2006
CARD 06-21640; Unnecessary Contamination of Personnel; dated March 29, 2006
CARD 06-21639; Evaluate Dose an Dose Rate Alarms for Fast Entry Electronic Dosimeters;
CARD 06-21639; Evaluate Dose an Dose Rate Alarms for Fast Entry Electronic Dosimeters;
Line 1,739: Line 2,066:
Procedure 67.000.103; Survey of Outgoing Radioactive Material Shipments; Revision 16
Procedure 67.000.103; Survey of Outgoing Radioactive Material Shipments; Revision 16
Procedure 67.000.102; Survey of Incoming Radioactive Material Shipments; Revision 0
Procedure 67.000.102; Survey of Incoming Radioactive Material Shipments; Revision 0
                                              8                                Attachment


                        LIST OF ACRONYMS USED
Attachment
ALARA As Low As Reasonable Achievable
9
CARD Condition Assessment Resolution Document
LIST OF ACRONYMS USED
CDF   Core Damage Frequency
ALARA
CFR   Code of Federal Regulations
As Low As Reasonable Achievable
CTG   Combustion Turbine Generator
CARD
DRP   Division of Reactor Projects
Condition Assessment Resolution Document
EDG   Emergency Diesel Generator
CDF
GSW   General Service Water
Core Damage Frequency
HPCI High Pressure Coolant Injection
CFR
IMC   Inspection Manual Chapter
Code of Federal Regulations
LER   Licensee Event Report
CTG
LERF Large Early Release Frequency
Combustion Turbine Generator
LLRT Local Leak Rate Test
DRP
MCC   Motor Control Center
Division of Reactor Projects
MSIV Main Steam Isolation Valve
EDG
NCV   Non-Cited Violation
Emergency Diesel Generator
NRC   Nuclear Regulatory Commission
GSW
PI   Performance Indicator
General Service Water
PMT   Post-Maintenance Testing
HPCI
RCIC Reactor Core Isolation Cooling
High Pressure Coolant Injection
RCS   Reactor Coolant System
IMC
RHR   Residual Heat Removal
Inspection Manual Chapter
RHRSW Residual Heat Removal Service Water
LER
RPS   Reactor Protection System
Licensee Event Report
RPSMG Reactor Protection System Motor Generator
LERF
RPT   Radiation Protection Technician
Large Early Release Frequency
RWCU Reactor Water Cleanup
LLRT
RWP   Radiation Work Package
Local Leak Rate Test
SCFH Standard Cubic Feet Per Hour
MCC
SCFM Standard Cubic Feet Per Minute
Motor Control Center
SDP   Significance Determination Process
MSIV
SGTS Standby Gas Treatment System
Main Steam Isolation Valve
SLC   Standby Liquid Control
NCV
SPAR Standardized Plant Analysis Risk
Non-Cited Violation
SRA   Senior Reactor Analyst
NRC
TM   Temporary Modifications
Nuclear Regulatory Commission
TS   Technical Specifications
PI
UFSAR Updated Final Safety Analysis Report
Performance Indicator
WR   Work Request
PMT
                                      9        Attachment
Post-Maintenance Testing
RCIC
Reactor Core Isolation Cooling
RCS
Reactor Coolant System
RHR
Residual Heat Removal
RHRSW
Residual Heat Removal Service Water
RPS
Reactor Protection System  
RPSMG
Reactor Protection System Motor Generator
RPT
Radiation Protection Technician
RWCU
Reactor Water Cleanup  
RWP
Radiation Work Package
SCFH
Standard Cubic Feet Per Hour  
SCFM
Standard Cubic Feet Per Minute
SDP
Significance Determination Process
SGTS
Standby Gas Treatment System
SLC
Standby Liquid Control
SPAR
Standardized Plant Analysis Risk
SRA
Senior Reactor Analyst
TM
Temporary Modifications
TS
Technical Specifications
UFSAR
Updated Final Safety Analysis Report
WR
Work Request
}}
}}

Latest revision as of 07:34, 15 January 2025

IR 05000341-06-003; 04/01/2006-06/30/2006; Fermi Power Plant, Unit 2; Fire Protection, Maintenance Risk Assessment, Operability Evaluations, Refueling and Outage Activities
ML062160540
Person / Time
Site: Fermi DTE Energy icon.png
Issue date: 08/02/2006
From: Christine Lipa
NRC/RGN-III/DRP/RPB4
To: Cobb D
Detroit Edison
References
IR-06-003
Download: ML062160540 (48)


See also: IR 05000341/2006003

Text

August 2, 2006

Mr. Donald K. Cobb

Assistant Vice President

Nuclear Generation

Detroit Edison Company

6400 North Dixie Highway

Newport, MI 48166

SUBJECT:

FERMI POWER PLANT, UNIT 2, NRC INTEGRATED

INSPECTION REPORT 05000341/2006003

Dear Mr. Cobb:

On June 30, 2006, the U.S. Nuclear Regulatory Commission (NRC) completed an integrated

inspection at your Fermi Power Plant, Unit 2. The enclosed report documents the inspection

findings which were discussed on July 11, 2006, with you and other members of your staff.

The inspection examined activities conducted under your license as they relate to safety and to

compliance with the Commissions rules and regulations and with the conditions of your license.

The inspectors reviewed selected procedures and records, observed activities, and interviewed

personnel.

Based on the results of this inspection, five findings of very low safety significance were

identified, all of which involved violations of NRC requirements. However, because these

findings were of very low safety significance and because the issues were entered into your

corrective program, the NRC is treating these findings as Non-Cited Violations in accordance

with Section VI.A.1 of the NRCs Enforcement Policy. If you contest the subject or severity of

a Non-Cited Violation, you should provide a response within 30 days of the date of this

inspection report, with the basis for your denial, to the U.S. Nuclear Regulatory Commission,

ATTN: Document Control Desk, Washington, DC 20555-0001, with a copy to the Regional

Administrator, U.S. Nuclear Regulatory Commission - Region III, 2443 Warrenville Road,

Suite 210, Lisle, IL 60532-4352; the Director, Office of Enforcement, U.S. Nuclear Regulatory

Commission, Washington, DC 20555-0001; and the Resident Inspector Office at the Fermi 2

facility.

In accordance with 10 CFR 2.390 of the NRCs Rules of Practice, a copy of this letter and

its enclosure will be made available electronically for public inspection in the NRC Public

D. Cobb

-2-

Document Room or from the Publicly Available Records (PARS) component of NRCs

document system (ADAMS). ADAMS is accessible from the NRC Web site at

http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room).

Sincerely,

/RA/

Christine A. Lipa, Chief

Branch 4

Division of Reactor Projects

Docket No. 50-341

License No. NPF-43

Enclosure:

Inspection Report 05000341/2006003

w/Attachment: Supplemental Information

cc w/encl:

K. Hlavaty, Plant Manager

R. Gaston, Manager, Nuclear Licensing

D. Pettinari, Legal Department

Michigan Department of Environmental Quality

Waste and Hazardous Materials Division

M. Yudasz, Jr., Director, Monroe County

Emergency Management Division

Supervisor - Electric Operators

State Liaison Officer, State of Michigan

Wayne County Emergency Management Division

D. Cobb

-2-

Document Room or from the Publicly Available Records (PARS) component of NRCs

document system (ADAMS). ADAMS is accessible from the NRC Web site at

http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room).

Sincerely,

Christine A. Lipa, Chief

Branch 4

Division of Reactor Projects

Docket No. 50-341

License No. NPF-43

Enclosure:

Inspection Report 05000341/2006003

w/Attachment: Supplemental Information

cc w/encl:

K. Hlavaty, Plant Manager

R. Gaston, Manager, Nuclear Licensing

D. Pettinari, Legal Department

Michigan Department of Environmental Quality

Waste and Hazardous Materials Division

M. Yudasz, Jr., Director, Monroe County

Emergency Management Division

Supervisor - Electric Operators

State Liaison Officer, State of Michigan

Wayne County Emergency Management Division

DOCUMENT NAME:E:\\Filenet\\ML062160540.wpd

G Publicly Available

G Non-Publicly Available

G Sensitive

G Non-Sensitive

To receive a copy of this document, indicate in the concurrence box "C" = Copy without attach/encl "E" = Copy with attach/encl "N" = No copy

OFFICE

RIII

RIII

NAME

RLerch:dtp

CLipa

DATE

08/02/06

08/02/06

OFFICIAL RECORD COPY

Donald K. Cobb

-3-

ADAMS Distribution:

LXR1

DHJ

RidsNrrDirsIrib

GEG

KGO

RMM3

CAA1

LSL (electronic IRs only)

C. Pederson, DRS (hard copy - IRs only)

DRPIII

DRSIII

PLB1

TXN

ROPreports@nrc.gov (inspection reports, final SDP letters, any letter with an IR number)

Enclosure

U. S. NUCLEAR REGULATORY COMMISSION

REGION III

Docket No:

50-341

License No:

NPF-43

Report No:

05000341/2006003

Licensee:

Detroit Edison Company

Facility:

Fermi Power Plant, Unit 2

Location:

Newport, Michigan

Dates:

April 1 through June 30, 2006

Inspectors:

R. Michael Morris, Senior Resident Inspector

T. Steadham, Resident Inspector

A. Wilson, NRC Headquarters

M. Franke, Senior Resident Inspector, Perry

M. Jordan, NRC Consultant

R. Langstaff, Senior Reactor Inspector

M. Mitchell, Radiation Specialist

Approved by:

C. Lipa, Chief

Branch 4

Division of Reactor Projects

Enclosure

2

SUMMARY OF FINDINGS

IR 05000341/2006003; 04/01/2006-06/30/2006; Fermi Power Plant, Unit 2; Fire Protection,

Maintenance Risk Assessment, Operability Evaluations, Refueling and Outage Activities.

This report covers a 3-month period of inspection by resident inspectors and announced

baseline inspections by a regional radiation specialist inspector. Five Green findings, all of

which were associated with non-cited violations (NCVs) were identified. The significance of

most findings is indicated by their color (Green, White, Yellow, Red) using Inspection

Manual Chapter 0609, Significance Determination Process (SDP). Findings for which the

SDP does not apply may be Green after NRC management review. The NRCs program for

overseeing the safe operation of commercial nuclear power reactors is described in

NUREG-1649, Reactor Oversight Process, Revision 3, dated July 2000.

A.

NRC-Identified and Self-Revealed Findings

Cornerstone: Initiating Events

Green. The inspectors identified an NCV of 10 CFR 50.65(a)(4) for the failure to

perform an adequate risk assessment for the Division I battery load test. The licensee

failed to consider the effect the test would have on the temperature in the reactor

protection system motor generator set rooms. Consequently, the load bank used for the

test caused the room temperature to increase which necessitated the unanticipated

installation of a temporary fan to cool the room. The licensee entered this issue into

their corrective action program to evaluate any programmatic or procedural deficiencies

that may have contributed to this event.

This finding is more than minor because the licensees risk assessment failed to

consider maintenance activities that could increase the likelihood of an initiating event,

specifically a loss of shutdown cooling from a reactor protection system motor generator

set trip on high temperature. The finding is of very low safety significance because it did

not affect the ability of operators to recover from a loss of shutdown cooling if it had

occurred. The cause of the finding is related to the cross-cutting element of Human

Performance. (Section 1R13.2)

Cornerstone: Mitigating Systems

Green. The inspectors identified an NCV of license condition 2.C(9) due to the

presence of unauthorized transient combustible materials in the residual heat removal

complex. An office chair and a plastic trash bin half filled with paper were secured next

to the electrical panel and associated cable raceway for emergency diesel generator 12

ventilation in the emergency diesel generator 12 switchgear room. The licensee entered

this issue into their corrective action program and removed the unauthorized transient

combustible materials from the residual heat removal complex.

This finding is more than minor because it affected the Mitigating Systems Cornerstone

attribute for protection against external factors. Specifically, a fire involving the

unauthorized transient combustibles could have affected a nearby electrical panel and

associated cable raceway containing mitigating system equipment important to safety.

Enclosure

3

The finding is of very low safety significance because the unauthorized transient

combustible materials would not have ignited from existing sources of heat or electrical

energy. The cause of the finding is related to the cross-cutting element of Problem

Identification and Resolution. (Section 1R05.2)

Green. The inspectors identified an NCV of Technical Specification 3.1.5.a.2,

Amendment 38, for the standby liquid control (SLC) system being inoperable for longer

than the allowed time without the plant being placed in hot shutdown. The licensee

failed to properly evaluate the operability of SLC during sparging activities when the

issue was raised in 1999. As a result, the licensee initiated a 21-hour sparge on the

SLC tank on August 24, 1999, and failed to take actions in accordance with the

Technical Specifications. After the deficient evaluation was identified on June 1, 2006,

the licensee revised the applicable procedures to declare the SLC system inoperable

during sparging the SLC tank. The licensee entered this issue into their corrective

action program.

This finding is more than minor because it represented a programmatic deficiency in the

licensees chemical control program which affected the ability of the fire brigade to

respond to and mitigate the effects of a fire. Upon management review, the finding is of

very low safety significance because the quantities of the relevant chemicals were low

and the storage location was sufficiently remote from mitigating equipment.

(Section 1R05.3)

Cornerstone: Emergency Preparedness

Green. The inspectors identified an NCV of license condition 2.C(9), for the failure to

appropriately store chemicals in accordance with the fire hazards analysis. The licensee

failed to evaluate the fire fighting response guidelines in NFPA-49 for various chemicals

brought into the protective area and, therefore, failed to appropriately store them as

required by the licensees fire hazards analysis. As a result, five normally stored

chemicals in the building have recommended fire fighting strategies that are inconsistent

with the licensees approved fire protection pre-plan. The licensee entered this issue

into their correction action program.

This finding is more than minor because it affected the equipment performance attribute

of the reactor safety cornerstone objective of ensuring the availability, reliability, and

capability of mitigating equipment to respond to initiating events to prevent undesirable

consequences. The finding is of very low safety significance because the total time of

sparging activities was short. (Section 1R15.2)

Cornerstone: Occupational Radiation Safety

Green. A self-revealed NCV was identified for the licensees failure to comply with

Technical Specification 5.4.1.a, written procedures shall be established, implemented,

and maintained covering applicable procedures recommended in Regulatory

Guide 1.33. The licensee did not adequately control the modification of the ventilation

equipment used to vent airborne radioactive particulate to the refuel floor during reactor

vessel floodup. Consequently, while raising reactor vessel water level, the improper

venting led to personnel contaminations, uptakes of radioactive material, and the

Enclosure

4

evacuation of the Reactor Building. The licensee entered this issue into their corrective

action program and conducted an investigation into the event. The corrective actions

recommended the development and implementation of an acceptable methodology for

raising reactor water level.

This finding is more than minor because it affected the Occupational Radiation Safety

Cornerstone of Radiation Safety due to individual worker unplanned, unintended dose.

The finding was evaluated using the SDP and was determined to be a finding of very

low safety significance because there was not a substantial potential for overexposure

and the licensees ability to assess dose was not compromised. (Section 1R20)

B.

Licensee-Identified Violations

A violation of very low safety significance, which was identified by the licensee, has been

reviewed by the inspectors. Corrective actions taken or planned by the licensee have

been entered into the licensees corrective action program. This violation and corrective

actions are listed in Section 4OA7 of this report.

Enclosure

5

REPORT DETAILS

Summary of Plant Status

Unit 2 began this inspection period shutdown for refueling outage 11 (RF11). Reactor

startup began on May 3 but was halted at 95 percent power on May 9 due to indications

of a fuel leak. Suppression testing commenced that same day, reducing reactor power

to approximately 63 percent until May 12 when the operators began increasing reactor

power after suppressing the fuel leak. On May 14, the reactor was at full power where it

remained at or near until May 19 when the operators began a reactor shutdown to

replace the leaking fuel assembly. After completing the work, operators began a reactor

startup on May 28. The reactor reached full power on May 30 where it remained at or

near until June 15 when an automatic reactor scram occurred as a result of a failure of

main unit transformer 2B. The failed transformer was disconnected and reactor startup

began on June 16. On June 21, the reactor reached 63 percent power (maximum

planned with transformer 2B out of service) and remained there for the remainder of the

inspection period.

1.

REACTOR SAFETY

Cornerstone: Mitigating Systems, Barrier Integrity, Initiating Events, Emergency

Preparedness

1R01

Adverse Weather (71111.01A)

a.

Inspection Scope

The inspectors reviewed licensee procedures for mitigating the effects of hot weather.

The inspectors reviewed severe weather procedures, emergency plan implementing

procedures related to severe weather, and annunciator response procedures, and

performed walkdowns. This included the reactor building and turbine building ventilation

preparations. Additionally, the inspectors reviewed condition assessment resolution

documents (CARD) and verified problems associated with adverse weather were

entered into the corrective action program with the appropriate significance

characterization.

These activities represented one hot weather systems preparation inspection sample.

b.

Findings

No findings of significance were identified.

Enclosure

6

1R04

Equipment Alignments (71111.04)

.1

Partial System Walkdowns (71111.04Q)

a.

Inspection Scope

The inspectors performed partial system walkdowns of the following risk-significant

systems:

C

Safety Relief Valves performed the week of April 3, 2006;

C

SLC A performed the week of April 24, 2006;

C

Division II Residual Heal Removal (RHR) and Residual Heat Removal Service

Water (RHRSW) Lineup performed the week of May 14, 2006;

C

Standby Electrical Power (emergency diesel generator [EDG]) lineup performed

the week of May 14, 2006; and

C

Division I RHR and RHRSW Shutdown Cooling performed the week of

May 21, 2006.

The inspectors selected these systems based on their risk significance relative to the

reactor safety cornerstones. The inspectors reviewed operating procedures, system

diagrams, Technical Specification (TS) requirements, Administrative TS, and the impact

of ongoing work activities on redundant trains of equipment in order to identify

conditions that could have rendered the systems incapable of performing their intended

functions. The inspectors also walked down accessible portions of the systems to verify

system components were aligned correctly.

In addition, the inspectors verified equipment alignment problems were entered into the

corrective action program with the appropriate significance characterization.

These activities represented five quarterly partial system walkdown inspection samples.

b.

Findings

No findings of significance were identified.

.2

Complete System Walkdown (71111.04S)

a.

Inspection Scope

The inspectors performed a complete system walkdown of the following risk-significant

system:

General Service Water (GSW) performed the week of April 24, 2006

The inspectors reviewed operating procedures, system diagrams, TS requirements, and

applicable sections of the Updated Final Safety Analysis Report (UFSAR) to ensure the

correct system lineup. The inspectors verified acceptable material condition of system

components, availability of electrical power to system components, and that ancillary

equipment or debris did not interfere with system performance.

Enclosure

7

These activities represented one semi-annual complete system walkdown inspection

sample.

b.

Findings

No findings of significance were identified.

1R05

Fire Protection (71111.05)

.1

Routine Resident Inspector Tours (71111.05Q)

a.

Inspection Scope

The inspectors conducted fire protection tours of the following risk-significant plant

areas:

Condensate Pump Room;

Standby Gas Treatment, Pipe Room;

Top of Torus;

RHR Complex, Division I RHR;

RHR Complex, Division I EDG, Switchgear Rooms, Ventilation Rooms;

RHR Complex, Division I RHRSW Pump Room;

Hemyc Wrap for the Fire Barrier;

Division I, RHR Pump Room;

Division II, RHR Pump Room;

Main Unit Transformer 2B; and

Division II Electrical Switchgear Room.

The inspectors verified fire zone conditions were consistent with assumptions in the

licensee's fire hazards analysis. The inspectors walked down fire detection and

suppression equipment, assessed the material condition of fire fighting equipment, and

evaluated the control of transient combustible materials. In addition, the inspectors

verified fire protection related problems were entered into the corrective action program

with the appropriate significance characterization.

These activities represented eleven routine quarterly fire protection inspection samples.

b.

Findings

No findings of significance were identified.

.2

RHR Complex, Division II EDG, Switchgear and Ventilation Rooms

a.

Inspection Scope

The inspectors also conducted fire protection tours of the RHR complex, Division II

EDG, switchgear and ventilation rooms which are risk-significant plant areas.

Enclosure

8

The inspectors verified fire zone conditions were consistent with assumptions in the

licensee's fire hazards analysis. The inspectors walked down fire detection and

suppression equipment, assessed the material condition of fire fighting equipment, and

evaluated the control of transient combustible materials. In addition, the inspectors

verified fire protection related problems were entered into the corrective action program

with the appropriate significance characterization.

These activities represented one routine quarterly fire protection inspection sample.

b.

Findings

Introduction: The inspectors identified an NCV of license condition 2.C(9) having very

low safety significance (Green) for the presence of unauthorized transient combustible

materials in the RHR complex.

Description: On May 15, 2006, the inspectors identified unauthorized transient

combustible materials in the RHR complex EDG 12 switchgear room. Specifically, the

inspectors identified an office chair and a plastic trash bin approximately half full of

paper secured approximately one foot from panel H21-P351, a safety-related electrical

panel for EDG 12 room ventilation, and associated cable raceway.

Section 9A.1.3.2.e of the UFSAR stated that the fire protection program had a

component to minimize the amount of combustibles to which safety-related areas may

be exposed. Procedure MOP11 implemented the fire protection program by prescribing

methods for controlling transient combustible material and the location of plant support

equipment. Step 3.5.1 of procedure MOP11 required a Plant Support Equipment

Approval form be obtained before placing any support equipment in the RHR complex.

The procedural requirement existed to ensure the introduction of transient combustible

materials was reviewed by fire protection personnel. However, no Plant Support

Equipment Approval form was submitted for the chair and trash bin identified in the

EDG 12 switchgear room within the RHR complex.

After the inspectors informed the fire protection supervisor of the issue, the fire

protection supervisor initiated CARD 06-23388 to initiate corrective actions. Licensee

personnel performed a walkdown of the RHR complex and identified three additional

trash bins and two chairs in other switchgear rooms within the RHR complex. The trash

bins and chairs were removed from the switchgear rooms.

Analysis: The inspectors determined the licensees failure to properly control transient

combustibles was a performance deficiency because the licensee is expected to comply

with their fire hazards analysis and because it was within the licensees ability to foresee

and prevent. The finding was greater than minor in accordance with Inspection Manual

Chapter (IMC) 0612, Power Reactor Inspection Reports, Appendix B, Issue

Disposition Screening, issued September 30, 2005, because the finding affected the

Mitigating Systems Cornerstone attribute for protection against external factors, i.e., fire.

Specifically, a fire involving the unauthorized transient combustibles could have affected

a nearby electrical panel and associated cable raceway containing mitigating system

equipment important to safety. The inspectors identified that a credible fire scenario

existed in that equipment important to safety was located within the zone of influence of

Enclosure

9

the unauthorized transient combustible materials as described by Table 2.3.2,

Calculated Values (in feet) for Use in the Ball and Column Zone of Influence Chart for

Fires in an Open Location Away from Walls of IMC 0609, Appendix F, Fire Protection

Significance Determination Process, issued February 28, 2005.

The inspectors completed a significance determination of this issue using IMC 0609,

Appendix FProperty "Inspection Manual Chapter" (as page type) with input value "NRC Inspection Manual 0609,</br></br>Appendix F" contains invalid characters or is incomplete and therefore can cause unexpected results during a query or annotation process.. The inspectors reviewed IMC 0609, Appendix F, Attachment 2,

Degradation Rating Guidance Specific to Various Fire Protection Program Elements,

and determined the unauthorized transient combustible materials represented a low

degradation rating because the materials would not have ignited from existing sources

of heat or electrical energy. As such, the finding screened to Green under Question 1 of

IMC 0609, Appendix F, Task 1.3.1, Qualitative Screening for All Finding Categories,

and was considered a finding of very low safety significance. The primary cause of this

finding was related to the cross-cutting aspect of problem identification and resolution

because the licensees response to several recent instances of unauthorized transient

combustibles was not effective in preventing this instance of unauthorized transient

combustibles.

Enforcement: License condition 2.C.(9) required the licensee to implement and

maintain in effect all provisions of the approved fire protection program as described in

the UFSAR. Section 9A.1.3.2.e of the UFSAR stated the fire protection program had a

component to minimize the amount of combustibles to which safety-related areas may

be exposed. Procedure MOP11 implemented the fire protection program by prescribing

methods for controlling transient combustible material and the location of plant support

equipment. Step 3.5.1 of procedure MOP11 required a Plant Support Equipment

Approval form be obtained before placing any support equipment in the RHR complex, a

safety-related area. Contrary to the above, on May 15, 2006, the inspectors identified

support equipment, i.e., a chair and a trash bin, had been placed in the EDG 12

switchgear room within the RHR complex without a Plant Support Equipment Approval

form having been obtained. Once identified, the licensee initiated CARD 06-23388,

performed a walkdown of the RHR complex, and removed unauthorized chairs and trash

bins from the switchgear rooms in the RHR complex. Because this violation is of very

low safety significance and because it was entered into the licensees corrective action

program as CARD 06-23388, this violation is being treated as an NCV, consistent with

Section VI.A.1 of the NRC Enforcement Policy: NCV 05000341/2006003-01:

Unauthorized Transient Combustibles in Safety-Related Areas.

.3

Fire Protection - Drill Observation (71111.05A)

a.

Inspection Scope

The inspectors assessed fire brigade performance and the drill evaluators' critique

during an unannounced fire brigade drill on June 21, 2006. The drill simulated a fire in

the chemical storage room in the radioactive waste building. The inspectors focused on

the command and control of fire brigade activities, fire fighting and communication

practices, material condition and use of fire fighting equipment, and implementation and

adequacy of pre-planned fire fighting strategies.

Enclosure

10

These activities represented one annual fire protection - drill observation inspection

sample.

b.

Findings

Introduction: The inspectors identified a Green NCV of license condition 2.C(9) for the

failure to appropriately store chemicals in accordance with the fire hazards analysis.

Description: The inspectors watched Fire Brigade Drill Scenario Number 6 which

involved a simulated fire in the chemical storage room on the first floor of the radioactive

waste building. Firefighters entered the room wearing full protective clothing and

positive-pressure, self-contained breathing apparatus. In accordance with fire protection

Pre-Plan FP-RDWST, Rev. 4, Radioactive Waste Building Zones 22, 23, 24, and 25, the

brigade simulated extinguishing the fire by using a water hose in a fog pattern.

The inspectors later questioned the adequacy of the fire protection pre-plan because it

did not appear to take into account differences in fire fighting strategies with the various

types of chemicals in the room. After reviewing the list of chemicals in the room against

the fire fighting strategies recommended by NFPA-49, Hazardous Chemicals Data 1994

Edition, the inspectors identified four chemicals normally stored in the room where

NFPA-49 recommends using special protective clothing when fighting a fire involving

those chemicals: monoethylamine solution, sodium hydroxide, potassium hydroxide,

and sulfuric acid. Additionally, NFPA-49 recommends against the use of water when

fighting fires involving sulfuric acid.

The inspectors reviewed the storage locations of these chemicals and determined they

were not segregated in such a manner to ensure a fire in that room did not involve any

of those chemicals. Further, the fire protection pre-plan contained no guidance on any

special precautions to be followed when fighting a fire involving any of those four

chemicals. The inspectors determined it was unreasonable to assume the responding

fire brigade would be able to easily determine what chemicals were on fire given the lack

of labeling and amount of smoke that likely would be present in the room during an

actual fire.

The licensees fire hazards analysis, as documented in UFSAR, Section 9A.5.G.3,

required chemicals be stored in accordance with the guidelines of NFPA-49. Although

the literal storage requirements for these chemicals were generally adhered to, e.g.,

stored in a cool, dry, ventilated room in metal cabinets, etc., the inspectors determined

the fire fighting strategies for the four chemicals of interest above were inseparable from

the storage guidelines because the licensee is expected to take all relevant information

into account when determining the appropriate chemical storage requirements. For

example, although NFPA-49 contained no guidance to store sulfuric acid separately

from nitric acid, the fact that water is suitable for fires involving nitric acid but not for fires

involving sulfuric acid logically concludes either, a) water should not be used if the

chemicals are in the same cabinet, b) the sulfuric acid should be stored in a separate

container, or c) the quantity of sulfuric acid is controlled sufficiently low so as to not

require segregation; none of which occurred. Likewise, because chemical suits are

recommended for those four chemicals but standard fire fighter turnout gear is suitable

for all other normally stored chemicals in the room, it is reasonable to expect the

Enclosure

11

licensee will take the emergency response personal protective equipment guidelines into

account when storing chemicals which the licensee also failed to do.

The inspectors questioned the licensee on how chemicals were controlled such that they

did not adversely affect the fire protection strategy and were informed that chemicals

are evaluated based on the effect they would have on the plant but not on the effect

they would have on fire fighting techniques. For example, there were no controls in

place to either ensure the fire brigade did not use water on fires involving sulfuric acid or

to control the amount of sulfuric acid below some threshold to preclude any alteration in

the fire fighting strategy.

Analysis: The inspectors determined the licensees failure to properly store chemicals in

accordance with guidelines contained in NFPA 49 was a performance deficiency

because the licensee is expected to comply with their fire hazards analysis and because

it was within the licensees ability to foresee and prevent. The finding is more than

minor because it represented a programmatic deficiency in the licensees chemical

control program which affected the ability of the fire brigade to respond to and mitigate

the effects of a fire. This finding affected the emergency planning cornerstone because

it affected the ability of the fire brigade to respond to a fire which could potentially affect

the licensees emergency plan.

The finding is not suitable for SDP evaluation, but has been reviewed by NRC

management and is determined to be a finding of very low safety significance (Green)

because the quantities of the relevant chemicals were low and the storage location was

sufficiently remote from mitigating equipment.

Enforcement: Fermi 2 Facility Operating License NPF-43, condition 2.C(9), required,

in part, that the licensee implement and maintain in effect all provisions of the

approved fire protection program as described in Section 9A of the UFSAR as

amended and approved in the Fermi 2 safety evaluation report through supplement 6.

UFSAR 9A.5.G.3 required hazardous chemicals be stored in accordance with the

guidelines of NFPA 49-1994, Hazardous Chemicals Data 1994 Edition. Contrary to

the above, on June 21, 2006, the licensee failed to utilize the guidelines contained in

NFPA 49-1994 when storing chemicals in the radioactive waste building. Because

this violation is of very low safety significance and because it was entered into the

licensees corrective action program as CARD 06-24243, this violation is being

treated as an NCV, consistent with Section VI.A.1 of the NRC Enforcement Policy:

NCV 05000341/2006003-02: Improper Storage of Chemicals Affecting Fire Fighting

Response.

1R06

Flood Protection (71111.06)

a.

Inspection Scope

The inspectors performed an inspection related to the licensee's precautions to mitigate

the risk from internal flooding events. The inspectors performed a walkdown of the

following plant areas to assess the adequacy of watertight doors and verify drains and

sumps were clear of debris and were operable:

Enclosure

12

High Pressure Coolant Injection Pump Room;

Reactor Core Isolation Cooling Pump Room;

Division I Core Spray Pump Room;

Division II Core Spray Pump Room; and

Auxiliary Building T Room.

The inspectors also reviewed the work activities associated with internal flooding to

verify identified problems were being entered into the corrective action program with the

appropriate characterization and significance.

These activities represented one internal flood protection inspection sample.

b.

Findings

No findings of significance were identified.

1R07

Heat Sink Performance (71111.07A)

a.

Inspection Scope

The inspectors reviewed completed test reports and observed the performance of

inspections for the RHR service water heat exchanger.

The inspectors selected this heat exchanger because its associated systems were risk

significant in the licensee's risk assessment and were required to support the operability

of other risk-significant, safety-related equipment. During these inspections, the

inspectors observed the as-found condition of the heat exchanger and verified no

deficiencies existed that would mask degraded performance. The inspectors discussed

the as-found condition as well as the historical performance of the heat exchanger with

engineering department personnel and reviewed applicable documents and procedures.

In addition, the inspectors verified heat sink problems were entered into the corrective

action program with the appropriate significance characterization, and completed

corrective actions were adequate and appropriately implemented.

These activities represented one heat sink performance inspection sample.

b.

Findings

No findings of significance were identified.

1R11

Licensed Operator Requalification (71111.11Q)

a.

Inspection Scope

On June 13, 2006, the inspectors observed an operations support crew during the

annual requalification examination in mitigating the consequences of events in

SS-OP-802-330, Anticipated Transient Without Scram with Small Steam Leak, Rev. 0,

dated January 26, 2006, on the simulator. The inspectors evaluated the following areas:

Enclosure

13

C

licensed operator performance;

C

crews clarity and formality of communications;

ability to take timely actions in the conservative direction;

prioritization, interpretation, and verification of annunciator alarms;

correct use and implementation of abnormal and emergency procedures;

C

control board manipulations;

C

oversight and direction from supervisors; and

C

ability to identify and implement appropriate TS actions and Emergency Plan

actions and notifications.

The crews performance in these areas was compared to pre-established operator

action expectations and successful critical task completion requirements.

These activities represented one quarterly licensed operator requalification inspection

sample.

b.

Findings

No findings of significance were identified.

1R12

Maintenance Effectiveness (71111.12Q)

a.

Inspection Scope

The inspectors evaluated degraded performance issues involving the following three

risk-significant systems:

C

Station Blackout Diesel Generators CTG 11-1, 2, 3, 4, and 120 kV switchyard;

C

RHR System A and B; and

C

Molded Case Circuit Breakers.

The inspectors assessed performance issues with respect to the reliability, availability,

and condition monitoring of the system. Specifically, the inspectors independently

verified the licensee's actions to address system performance or condition problems in

terms of the following:

C

implementing appropriate work practices;

C

identifying and addressing common cause failures;

C

scoping of systems in accordance with 10 CFR 50.65(b);

C

characterizing system reliability issues;

C

tracking system unavailability;

C

trending key parameters (condition monitoring);

C

ensuring 10 CFR 50.65(a)(1) or (a)(2) classification and/or re-classification; and

C

verifying appropriate performance criteria for systems classified as (a)(2) and/or

appropriate and adequate goals and corrective actions for systems classified as

(a)(1).

In addition, the inspectors verified maintenance effectiveness issues were entered into

the corrective action program with the appropriate significance characterization.

Enclosure

14

These activities represented three quarterly maintenance effectiveness inspection

samples.

b.

Findings

No findings of significance were identified.

1R13 Maintenance Risk Assessments and Emergent Work Control (71111.13Q)

.1

Routine Maintenance Risk Assessments

a.

Inspection Scope

The inspectors reviewed the licensee's evaluation and management of plant risk for the

maintenance and operational activities affecting risk-significant and safety-related

equipment listed below:

maintenance risk for week of April 2, 2006;

maintenance risk for week of April 17, 2006;

maintenance risk for week of April 30, 2006; and

maintenance risk for week of June 26, 2006.

These activities were selected based on their potential risk significance relative to the

reactor safety cornerstones. As applicable for each activity, the inspectors reviewed the

scope of maintenance work, discussed the results of the assessment with the licensee's

probabilistic risk analyst and/or shift technical advisor, and verified plant conditions were

consistent with the risk assessment. The inspectors also reviewed TS requirements and

walked down portions of redundant safety systems, when applicable, to verify risk

analysis assumptions were valid and applicable requirements were met.

These activities represented four quarterly maintenance risk assessment and

emergency work control inspection samples.

b.

Findings

No findings of significance were identified.

.2

Inadequate Maintenance Risk Assessment

a.

Inspection Scope

The inspectors reviewed the activities surrounding the Division I battery load test

performed during RF11 to determine if the licensee appropriately considered the risk

impacts of performing the test. The inspectors interviewed licensee staff, reviewed

documents, and performed walkdowns. The inspectors considered ancillary equipment

affected by the test to determine what affect, if any, the test would have on it.

These activities represented one quarterly maintenance risk assessment and

emergency work control inspection sample.

Enclosure

15

b.

Findings

Introduction: The inspectors identified a Green NCV of 10 CFR 50.65(a)(4) for the

failure to perform an adequate risk assessment for the Division I battery load test.

Description: On April 3, 2006, the inspectors identified a temporary fan installed in the

blocked-open doorway to the dc motor control center (DC MCC) area. Upon entering

the room, the inspectors noticed that additional doors inside the DC MCC area leading

to each of the reactor protection system motor generator (RPSMG) set rooms were

open. After questioning why the doors were blocked open and a fan installed, the

inspectors learned operators took those actions to provide additional cooling to the

RPS MG sets because the Division I 130/260 VDC battery load surveillance test,

procedure 42.309.05, was in progress.

Because the air-cooled load bank used for the test was temporarily installed in the

DC MCC area, temperatures in the room started to increase after the test commenced.

However, two area room coolers were out of service due to a scheduled outage of the

GSW system which left the DC MCC, vital battery, battery charger, and RPS MG set

rooms with no cooling. In order to help prevent a loss of shutdown cooling, which would

have occurred had the RPS MG sets tripped, the operators had previously blocked

opened the doors to the RPS MG set rooms which further increased the temperature in

the DC MCC area. Operators then blocked open the double doors to the DC MCC area

and installed a large utility fan in the doorway to provide additional cooling to the area.

The test was successfully completed, temperatures dropped, and the fan was removed.

The outage risk associated with this test did not consider the effects it would have on

the key safety function of maintaining decay heat available due to the additional heat

from the load bank with no room cooling. Moreover, the outage risk associated with the

GSW outage assumed that the RPS MG sets would not be running. Consequently,

prudent risk management actions were not developed prior to performing the battery

load test. However, because operators installed a fan in the open doorway early

enough into the test, shutdown cooling remained in operation.

Analysis: The inspectors determined the failure to perform an adequate risk analysis of

maintenance activities prior to performing maintenance was a performance deficiency

because the licensee is expected to comply with the requirements of the maintenance

rule. This finding is more than minor because the licensees risk assessment failed to

consider maintenance activities that could increase the likelihood of an initiating event,

specifically a loss of shutdown cooling. In addition, this finding affected the initiating

event cornerstone because it is associated with an increase in the likelihood of an

initiating event. The inspectors utilized the maintenance risk and shutdown risk SDP to

assess the risk of this finding. The finding is of very low safety significance because the

finding did not affect the ability of operators to recover from a loss of shutdown cooling

had it occurred. The inspectors determined the cause of this finding impacted the

Human Performance cross-cutting area because the cause of the inadequate risk

assessment was due to a personnel error.

Enforcement: 10 CFR 50.65(a)(4) requires, in part, that before performing

maintenance activities, the licensee shall assess and manage the increase in risk

Enclosure

16

that may result from the proposed maintenance activities. Contrary to the above,

beginning on April 1, 2006, and continuing through April 6, 2006, the licensee

performed surveillance procedure 42.309.05 without adequately assessing and

managing the increase in risk prior to performing the activity. Because this violation is

of very low safety significance and because it was entered into the licensees corrective

action program as CARD 06-21892 and 06-24495, this violation is being treated as an

NCV, consistent with Section VI.A.1 of the NRC Enforcement Policy:

NCV 05000341/2006003-03: Inadequate Maintenance Risk Assessment.

1R14

Personnel Performance During Non-Routine Plant Evolutions and Events (71111.14)

a.

Inspection Scope

The inspectors reviewed the licensees actions in response to the following non-routine

events to ensure the licensee took appropriate actions in accordance with licensee

procedures:

unplanned reactor building contamination, CARD 06-21534;

control rod position indication malfunction, CARD 06-23491 & 06-23489;

main turbine bypass valves opened at power, CARD 06-24113; and

mode 5 reactor scram during installation of shorting links, CARD 06-23588.

The inspectors reviewed operator logs, procedures, corrective action documents, other

documents, and interviewed personnel. The inspectors also evaluated the licensees

operational decision making involved with these non-routine events.

These activities represented four inspection samples.

b.

Findings

No findings of significance were identified.

1R15

Operability Evaluations (71111.15)

.1

Routine Review of Operability Evaluations

a.

Inspection Scope

The inspectors reviewed the following documents to ensure the identified condition did

not render the involved equipment inoperable or result in an unrecognized increase in

plant risk, and the licensee appropriately applied TS limitations and appropriately

returned the affected equipment to an operable status:

CARD 06-23114, Motor Operator Valve Motor Replacement for RHR Shutdown

Cooling Inboard Suction Bypass Valve; and

CARD 06-23898, Division II Emergency Equipment Cooling Water Makeup

Pump In-Service Test Flow Unattainable.

These activities represented two operability evaluation inspection samples.

Enclosure

17

b.

Findings

No findings of significance were identified.

.2

Standby Liquid Control Operability During Air Sparging Operations

a.

Inspection Scope

The inspectors reviewed the licensees practice of placing an air sparge on the SLC tank

to determine if system operability was justified. The inspectors reviewed previous

engineering evaluations to determine the technical adequacy of the conclusions. The

inspectors reviewed operator logs, TS, design basis documents, UFSAR, and other

documents. The inspectors interviewed operators, engineers, and other licensee staff.

These activities represented one operability evaluation inspection sample.

b.

Findings

Introduction: The inspectors identified a Green NCV of TS for the SLC system being

inoperable for longer than the action time to be in hot shutdown with both SLC

subsystems inoperable.

Description: In April 1999, the licensee reviewed an operating experience report issued

by another licensee discussing the inoperability of the SLC system during air sparging

activities. Air sparging the SLC tank was done to facilitate mixing of the sodium

pentaborate in the tank and was performed prior to the monthly chemistry analysis and

after any chemical addition to the tank. The air sparge header was located near the

bottom of the tank in proximity to the SLC pump suction line. The concern was that if

the pumps were operating while the air sparge was operating, air could be drawn into

the pumps and compromise their ability to perform their design function. The licensee

initiated CARD 99-13240 to evaluate the applicability of the issue to Fermi.

The licensee determined that although pump performance would be impacted if the

pumps were required while an SLC tank air sparge was in progress, the pumps

remained operable. Based on input from the pump vendor, the licensee concluded that

entrained air in the pumped water would cause increased pump vibration and a

negligible reduction in delivered flow rate. Because the vendor stated the increased

vibration would only affect long-term pump reliability, the licensee concluded that

long-term pump degradation was not a concern because SLC had a 2 hour2.314815e-5 days <br />5.555556e-4 hours <br />3.306878e-6 weeks <br />7.61e-7 months <br /> mission

time.

In an effort to lessen the probability of requiring the SLC pumps during an actual event

while the air sparge was operating, the licensee identified the need to revise the system

operating procedures to minimize duration of sparge operations from hours to minutes.

The action to revise procedure 23.149, Standby Liquid Control System, was originally

due on June 30, 1999.

The inspectors reviewed the licensees evaluation and noted the CARD did not contain

either any documentation from the vendor or any attempt to quantify the reduction in

Enclosure

18

flow rate to ensure the minimum required flow was maintained. The inspectors asked

the licensee for the vendors recommendations in writing but were later told the pump

vendor declined to support their previous conclusion in writing. The inspectors were

concerned that if the pump vendor was unwilling to state in writing that the pumps would

operate for at least 2 hours2.314815e-5 days <br />5.555556e-4 hours <br />3.306878e-6 weeks <br />7.61e-7 months <br /> during sparging, then pump operability was not justified.

The inspectors brought their concern to the licensee who entered the issue into their

corrective action program as CARD 06-23785 on June 1, 2006. After further review, the

licensee concluded that SLC operability during sparging could not be supported and

revised procedure 23.149 accordingly. Upon review of control room logs, the inspectors

determined that although the licensee significantly reduced the total sparging time since

1999, the tank was air sparged for 21 hours2.430556e-4 days <br />0.00583 hours <br />3.472222e-5 weeks <br />7.9905e-6 months <br /> on August 24, 1999, which exceeded the

time to be in hot shutdown of 20 hours2.314815e-4 days <br />0.00556 hours <br />3.306878e-5 weeks <br />7.61e-6 months <br /> with both SLC subsystems inoperable while in

Mode 1 or 2. In addition, the inspectors concluded the maximum unavailability in any

1-year period after identification of the issue in 1999 was approximately 90 hours0.00104 days <br />0.025 hours <br />1.488095e-4 weeks <br />3.4245e-5 months <br />.

Analysis: The inspectors determined the licensees failure to appropriately evaluate

SLC operability during sparging operations was a performance deficiency because the

licensee is expected to adequately evaluate issues that affect the operability of TS

equipment and because it was within the licensees ability to foresee and prevent. The

finding is more than minor because it affected the equipment performance attribute of

the reactor safety cornerstone objective of ensuring the availability, reliability, and

capability of mitigating equipment to respond to initiating events to prevent undesirable

consequences.

The inspectors assessed the finding using the SDP. Because the inspectors

considered this finding to represent an actual loss of a safety function of SLC, the

inspectors performed a phase 2 SDP analysis. A phase 3 analysis was subsequently

performed by the senior reactor analyst (SRA). The SRA performed the risk evaluation

using the Fermi Standardized Plant Analysis Risk (SPAR) Model, Level 1, Revision 3P,

Change 3.21, created October 2005. The SRA ran the SPAR model assuming common

cause failure of both SLC pumps, with an exposure time of 90 hours0.00104 days <br />0.025 hours <br />1.488095e-4 weeks <br />3.4245e-5 months <br />. Using the above

information the SRA obtained a change in core damage frequency (CDF) of 3.1E-8

(Green) for internal events. The dominant sequences involved a failure of the reactor to

scram after a transient, loss of condenser heat sink, and loss of main feedwater, and

failure of the SLC system.

Anticipated transient without scram events are not assumed to be caused by external

events and, therefore, the risk contribution from external events is insignificant.

Similarly, because the internal events CDF is less than 1E-7, large early release

frequency (LERF) is not significant per IMC 0609, Appendix H. The SRA concluded

the total CDF considering internal events, external events, and LERF is estimated at

3.1E-8 (Green).

Enforcement: Technical Specification 3.1.5.a.2, Amendment 38, required that while in

Modes 1 and 2, with the SLC system otherwise inoperable, the licensee must restore

the system to operable status within 8 hours9.259259e-5 days <br />0.00222 hours <br />1.322751e-5 weeks <br />3.044e-6 months <br /> or be in at least hot shutdown within the

next 12 hours1.388889e-4 days <br />0.00333 hours <br />1.984127e-5 weeks <br />4.566e-6 months <br /> and was in effect on August 24 and 25, 1999. Contrary to the above,

beginning on August 24, 1999, and continuing until August 25, 1999, while in Modes 1

Enclosure

19

and 2, the SLC system was inoperable for 21 hours2.430556e-4 days <br />0.00583 hours <br />3.472222e-5 weeks <br />7.9905e-6 months <br /> while the SLC tank was being air

sparged; therefore, on August 25, 1999, with the SLC system inoperable for greater

than 20 hours2.314815e-4 days <br />0.00556 hours <br />3.306878e-5 weeks <br />7.61e-6 months <br />, the plant was not in at least hot shutdown. Because this violation is of

very low safety significance and because it was entered into the licensees corrective

action program as CARD 06-23785, this finding is being treated as an NCV, consistent

with Section VI.A.1 of the NRC Enforcement Policy: NCV 05000341/2006003-04:

Improper Evaluation of Standby Liquid Control Operability During Tank Sparging.

.3

Inappropriate Use of Risk in Operability Evaluations

a.

Inspection Scope

The inspectors reviewed CARD 06-23913 to ensure that the identified condition did not

render the involved equipment inoperable or result in an unrecognized increase in plant

risk and that the licensee appropriately applied TS limitations and appropriately returned

the affected equipment to an operable status.

These activities represented one operability evaluation inspection sample.

Introduction: The inspectors identified an Unresolved Item (URI) when the licensee

removed pipe insulation, credited for environmental qualification of nearby equipment,

while at power without an adequate engineering evaluation.

Description: On June 8, 2006, the licensee initiated CARD 06-23913 to request a work

request to replace contaminated insulation on the suction and discharge pipe for the B

RHR pump. As a result, Work Request (WR) 000Z062027 was released and work

began on June 13, 2006. While performing a plant tour on June 15, 2006, the

inspectors identified the insulation was missing from the suction pipe for the B RHR

pump and questioned the licensee if the insulation removal had an approved

engineering evaluation. Because the equipment was in a potentially harsh environment,

the uninsulated pipe would increase the temperature profile of the room during accident

conditions which could affect the environmental qualification of electrical equipment in

the room. The licensee stated the evaluation was documented in CARD 06-23913 and

concluded that removing the insulation while at power was acceptable.

The inspectors reviewed the subject evaluation and became concerned that one of the

assumptions for the evaluation was that an accident was not considered as credible

during the period of time the insulation was to be removed. Upon further review, the

inspectors learned the licensee used non-accident heat loads to determine the

environmental effects of removing the insulation. The licensees justification was that if

the total time the insulation was removed was less than 168 hours0.00194 days <br />0.0467 hours <br />2.777778e-4 weeks <br />6.3924e-5 months <br />, then the probability

of either a high energy line break or loss of coolant accident was negligible and, hence,

did not need to be assumed to occur.

The definition of operability stated, however, the equipment must be capable of

performing its specified function(s). The inherent assumption was the occurrence,

conditions, or event would exist and the safety function could be performed. Therefore,

Enclosure

20

the inspectors concluded the use of probabilities of the occurrence of accidents while

the insulation was removed was an unacceptable assumption in the subsequent

operability evaluation.

While reviewing this evaluation, the inspectors discovered the licensee used the

same method of evaluating on-line insulation removal since at least September 20,

2001, and found five additional CARDs where the licensee approved removing

insulation from equipment in potentially harsh areas while at power, likewise with

unacceptable evaluations. Because the extent of condition of this issue is potentially

significant and could extend to work other than on-line insulation removal, this item is

unresolved pending the inspectors review of the licensees full extent of condition

review and subsequent risk evaluation and is identified as Unresolved Item

(URI) 05000341/2006003-05: Inappropriate Use of Risk in Operability Evaluations.

1R19

Post-Maintenance Testing (71111.19)

a.

Inspection Scope

The inspectors reviewed post-maintenance testing (PMT) activities associated with the

following scheduled maintenance:

Division I Switchyard Modifications, EDP 31880;

Feedwater Check Valve PMT, WR T210040100;

Drywell Cooler Number 4 Replacement, WR 000Z052131;

Reactor Core Isolation Cooling PMT;

Reactor Recirculation Pump Discharge Valve B310SF031A, Stem Replacement,

WR 000Z050487;

Main Steam Isolation Valve (MSIV), Limit Switch Replacement; and

WR 000Z060156, Replace Control Rod Drive Pump Inboard Bearing Oil Level

Sight glass.

The inspectors reviewed the scope of the work performed and evaluated the adequacy

of the specified PMT. The inspectors verified the PMT was performed in accordance

with approved procedures, the procedures clearly stated acceptance criteria, and the

acceptance criteria were met. The inspectors interviewed operations, maintenance, and

engineering department personnel and reviewed the completed PMT documentation.

In addition, the inspectors verified PMT problems were entered into the corrective action

program with the appropriate significance characterization.

These activities represented seven PMT inspection samples.

b.

Findings

No findings of significance were identified.

Enclosure

21

1R20

Refueling and Outage Activities (71111.20)

.1

Routine Refueling Outage Inspection Activities

a.

Inspection Scope

The inspectors observed the licensees performance during RF11, which was in

progress at the beginning of this inspection and concluded on May 5, 2006.

This inspection consisted of a review of the licensees outage schedule, safe shutdown

plan and administrative procedures governing the outage, periodic observations of

equipment alignment, and plant and control room outage activities. Specifically, the

inspectors determined whether the licensee effectively managed elements of shutdown

risk pertaining to reactivity control, decay heat removal, inventory control, electrical

power control, and containment integrity.

The inspectors performed the following activities daily, during the outage:

attended control room operator and outage management turnover meetings to

verify the current shutdown risk status was well understood and communicated;

performed walkdowns of the main control room to observe the alignment of

systems important to shutdown risk;

observed the operability of reactor coolant system (RCS) instrumentation and

compared channels and trains against one another;

performed walkdowns of the turbine, auxiliary, and reactor buildings and the

drywell to observe ongoing work activities, to ensure work activities were

performed in accordance with plant procedures, and to verify procedural

requirements regarding fire protection, foreign material exclusion, and the

storage of equipment near safety-related structures, systems, and components

were maintained;

verified the licensee maintained secondary containment in accordance with TS

requirements; and

reviewed selected issues the licensee entered into its corrective action program

to verify identified problems were being entered into the program with the

appropriate characterization and significance.

Additionally, the inspectors performed the following specific activities:

monitored refueling activities to verify the licensee adhered to established

procedures and TS requirements for handling of irradiated fuel;

performed drywell closeout;

verified shutdown cooling tagouts;

verified completion of restart restraint items; and

observed control rod withdrawal to criticality and portions of the plant power

ascension.

In particular, the inspectors reviewed the licensees restart restraint process and verified

the closure of selected issues. Documents reviewed during these inspection activities

are listed at the end of this report.

Enclosure

22

Because inspection activities for this refueling outage constituted one inspection sample

in Inspection Report 05000341/2006002, and since only one sample is counted per

outage, the inspection activities for this inspection period do not constitute an additional

refueling and outage inspection sample.

b.

Findings

Introduction: The inspectors identified a Green NCV of Technical Specification 5.4.1.a,

for the failure to adequately control the modification of the ventilation equipment used to

vent airborne radioactive particulate to the refuel floor during reactor vessel floodup.

Description: At 1450, on March 26, 2006, operators initiated core spray at approximately

3000 gpm to raise reactor water level, to permit removal of the reactor vessel head. The

reactor vessel head vent pipe had been disconnected, to permit installation of a

ventilation unit for the venting of gases to the refuel floor. The ventilation unit consisted

of a nominal 3600 scfm fan, a charcoal filter, and a HEPA particulate filter. Neither filter

had been recently tested. The ventilation unit was configured with two hoses placed to

take suction close to the reactor vessel head vent. The exhaust of the ventilation unit

ran to a point below an intake for the Standby Gas Treatment System (SGTS), to permit

capture of the exhaust by the SGTS.

At approximately 1500, the ventilation unit intake hoses were observed being pushed

away from the reactor vessel head vent, due to flow from the vent. Core spray was shut

down at 1502 and at 1504 visible moisture was seen being emitted from the vent. A

continuous air monitor on the refuel floor alarmed at 1510 and RP ordered the

evacuation of all but essential personnel from the refuel floor. By 1525 all personnel

were removed from the floor and shortly after this, the entire reactor building was

evacuated due to the spread of contamination. Decontamination of several workers was

required. Twenty-eight workers were whole body counted, with 26 showing uptakes of

varying levels of Co-60, Co-58, and Mn-54.

There were three conditions that contributed to the cause of the event. First of all,

coolant activity levels were higher than expected due to a crud burst during shutdown

and the temporary loss of RWCS allowed Co-60 to enter and remain in the coolant,

possibly plating out on reactor internals. The second condition related to the

temperature of the material vented from the reactor vessel head. Reactor vessel

outside shell temperatures indicated 215 degrees F, which equates to internal metal

temperatures above the atmospheric boiling point of water. This indicates that some of

the coolant flashed to steam as the level in the reactor vessel rose, which could increase

the carryover of coolant activity to the vented gas. The third condition was the

inadequate processing of vented material from the reactor vessel head. The venting of

the airborne radioactive particulate would not have resulted in building contamination

and personnel uptakes if the ventilation unit had effectively removed this material to the

SGTS.

The use of the ventilation system was not in accordance with its design configuration.

The ventilation system for previous outages had suction hoses connected to a hood that

was placed over the reactor vessel head vent, to improve the capture of vented material.

The use of the hood was discontinued due to its impact on water level instrumentation.

Enclosure

23

An engineering evaluation was not performed on the impact of the change in

configuration of the ventilation system. In addition, the exhaust arrangement from the

ventilation unit to the SGTS had not been evaluated for effectiveness. Licensee

Procedure MES12, Performing Temporary Modifications, requires the modification

process be followed and an evaluation be performed.

Furthermore, licensee procedural guidance did not exist for the overall process of taking

the operating reactor to a condition allowing fuel movement. The event could have been

prevented if appropriate acceptance criteria for allowable reactor vessel temperature

and coolant activity levels existed. Thus, the root cause of the event was determined to

be a procedural and programmatic weakness.

The licensee initiated CARD 06-21534, Continuous Air Monitor Alarm on Refueling

Floor, to track the investigation of the event in their CAP. The primary corrective action

recommendation is to develop and implement an acceptable methodology for raising

reactor vessel water level. In addition, the design and configuration of the current

ventilation exhaust capture system will be evaluated and modified, as appropriate to

assure that it is adequate for the expected reactor vessel fill rate and radioactive

material concentrations. The methodology may involve an alternate vent path, such as

using the attached piping to vent the reactor vessel to the drywell.

Analysis: The inspectors determined the licensees lack of control of the Temporary

Modification process constituted a design control issue. The licensees failure to

adequately control the process used to vent airborne radioactive particulate to the refuel

floor during reactor vessel floodup represents a performance deficiency as defined in

NRC Inspection Manual Chapter 0612, Appendix B, Issue Screening. The issue was

determined to be more than minor because if left uncorrected the issue could become a

more significant safety concern if coolant activity levels were higher or if the vessel was

flooded quicker.

The finding was assessed using NRC Inspection Manual Chapter 0609, Appendix C,

Occupational Radiation Safety Significance Determination Process due to individual

worker unplanned, unintended dose. The finding was determined to be of very low

safety significance because the inspectors answered, NO, to all four phase 1

screening questions.

Enforcement: Technical Specification 5.4.1.a requires that procedures recommended in

Regulatory Guide 1.33, Revision 2, Appendix A, February 1978, be established,

implemented and maintained. Section 4.a of that document, in part requires

instructions for filling, venting, and draining the reactor pressure vessel. Contrary to the

above, the initial installation of the ventilation system and the changes made to the

ventilation system that was used as part of the reactor vessel floodup during outages

was not processed through the Temporary Modification Procedure. This finding is being

treated as an NCV, consistent with Section VI.A.1 of the NRC Enforcement Policy and is

identified as NCV 05000341/2006003-06: Inadequate Controls for Venting the Reactor

Pressure Vessel Head. This issue is in the licensees corrective action program as

CARD 06-22667.

Enclosure

24

.2

Forced Outage 06-01

a.

Inspection Scope

The inspectors observed the licensees performance during Forced Outage 06-01 from

May 20, 2006, through May 29, 2006, which was scheduled to locate and replace a

failed fuel assembly. During power ascension following RF11, operators identified a

potential fuel leak because off gas radiation levels were slightly elevated from normal.

Operators began suppression testing later that day, which identified the failed assembly.

Operators initiated a manual unit shutdown to replace the failed fuel. While the unit was

shutdown, additional assemblies subjected to similar flux profile histories were also

replaced although fuel sipping operations identified only one fuel assembly with a fuel

cladding defect.

This inspection consisted of a review of the licensees outage schedule, safe shutdown

plan and administrative procedures governing the outage, periodic observations of

equipment alignment, and plant and control room outage activities. Specifically, the

inspectors determined whether the licensee effectively managed elements of shutdown

risk pertaining to reactivity control, decay heat removal, inventory control, electrical

power control, and containment integrity.

The inspectors performed the same daily activities, during the outage as described in

Section 1R20.1 for the refueling outage.

These activities represented one forced outage inspection sample.

b.

Findings

No findings of significance were identified.

.3

Forced Outage 06-02

a.

Inspection Scope

The inspectors observed the licensees performance during Forced Outage 06-02 from

June 15, 2006, through June 17, 2006. On June 15, a reactor scram occurred due to a

main turbine generator trip which occurred when main unit transformer 2B failed. The

inspectors responded to the control room and to the transformer area to assess the

licensees response to the event.

This inspection consisted of a review of the licensees outage schedule, safe shutdown

plan and administrative procedures governing the outage, and plant and control room

outage activities. Specifically, the inspectors determined whether the licensee

effectively managed elements of shutdown risk pertaining to reactivity control, decay

heat removal, inventory control, and electrical power control.

Enclosure

25

The inspectors performed the following activities during the outage:

attended control room operator and outage management turnover meetings to

verify the current shutdown risk status was well understood and communicated;

performed walkdowns of the main control room to observe the alignment of

systems important to shutdown risk;

observed the operability of RCS instrumentation and compared channels and

trains against one another; and

observed control rod withdrawal to criticality and portions of the plant power

ascension.

These activities represented one forced outage inspection sample.

b.

Findings

No findings of significance were identified.

1R22

Surveillance Testing (71111.22Q)

a.

Inspection Scope

The inspectors reviewed the test results for the following activities to determine whether

risk-significant systems and equipment were capable of performing their intended safety

function and to verify testing was conducted in accordance with applicable procedural

and TS requirements:

MSIV Limit Switch (routine);

SLC Squib Valve Test (routine);

Integrity Test for Containment Penetrations X-7A, X-7B, X-7C, and X-7D (LLRT);

Scram Nitrogen Accumulator Integrity Test (routine);

Scram Discharge Volume Vent and Drain Valves Operability (routine);

Secondary Containment Integrity Test (LLRT);

MSIV Channel Functional Test (isolation valve);

LOOP/LOCA Test (routine);

Reactor Core Isolation Cooling System Automatic Actuation and Flow Test

(routine); and

High Pressure Coolant Injection Flow Rate Test at 165 psig Reactor Steam

Pressure (routine).

The inspectors reviewed the test methodology and test results to verify equipment

performance was consistent with safety analysis and design basis assumptions. In

addition, the inspectors verified surveillance testing problems were being entered into

the corrective action program with the appropriate significance characterization.

These activities represented seven routine, two local leak rate test (LLRT), and one

containment isolation valve surveillance inspection samples.

Enclosure

26

b.

Findings

No findings of significance were identified.

1EP6 Drill Evaluation (71114.06)

a.

Inspection Scope

The inspectors observed the licensee perform classifications and protective action

recommendations during licensed operator requalification training on June 20, 2006.

The inspectors observed activities in the control room simulator. The inspectors also

attended the post-drill critique in the simulator. The focus of the inspectors activities

was to note any weaknesses and deficiencies in the shift managers performance as

emergency director and ensure the licensee evaluators noted the same weaknesses

and deficiencies and entered them into the corrective action program. As part of the

inspection, the inspectors reviewed the drill package included in the list of documents

reviewed at the end of this report.

These activities represented one drill evaluation inspection sample.

b.

Findings

No findings of significance were identified.

2OS1 Access Control to Radiologically Significant Areas (IP 71121.01)

.1

Plant Walkdowns and Radiation Work Permit Reviews

a.

Inspection Scope

The inspectors reviewed licensee controls and surveys in the following three

radiologically significant work areas within radiation areas, high radiation areas and

airborne radioactivity areas in the plant and reviewed work packages which included

associated licensee controls and surveys of these areas to determine if radiological

controls including surveys, postings and barricades were acceptable:

Turbine Building Main Steam Reheater Replacement;

Drywell Activities; and

Refuel Floor Activities.

These activities represented one inspection sample.

The inspectors reviewed the radiation work permits (RWPs) and work packages used to

access the three areas and other high radiation work areas to identify the work control

instructions and control barriers that had been specified. Electronic dosimeter alarm set

points for both integrated dose and dose rate were evaluated for conformity with survey

indications and plant policy. Workers were interviewed to verify they were aware of the

actions required when their electronic dosimeters noticeably malfunctioned or alarmed.

Enclosure

27

These activities represented one inspection sample.

The inspectors walked down and surveyed (using an NRC survey meter) the three areas

to verify the prescribed RWPs, procedure, and engineering controls were in place,

licensee surveys and postings were complete and accurate, and air samplers were

properly located.

These activities represented one inspection sample.

The inspectors reviewed RWPs for the following airborne radioactivity areas to verify

barrier integrity and engineering controls performance, e.g., high efficiency particulate

air filter ventilation system operation, and to determine if there was a potential for

individual worker internal exposures of greater than 50 millirem committed effective

dose equivalent. There were no areas where there was a potential for individual worker

internal exposures of greater than 50 millirem committed effective dose equivalent.

Work areas having a history of, or the potential for, airborne transuranic isotopes were

evaluated to verify the licensee had considered the potential for transuranic isotopes

and provided appropriate worker protection. There where no areas having a history of,

or the potential for, airborne transuranic isotopes.

These activities represented one inspection sample.

The adequacy of the licensees internal dose assessment process for any actual internal

exposures greater than 50 millirem committed effective dose equivalent was assessed.

There were no internal exposures greater than 50 millirem committed effective dose

equivalent.

These activities represented one inspection sample.

b.

Findings

No findings of significance were identified.

.2

Problem Identification and Resolution

a.

Inspection Scope

The inspectors reviewed three corrective action reports related to access controls and

high radiation area radiological incidents. Staff members were interviewed and

corrective action documents were reviewed to verify that follow-up activities were being

conducted in an effective and timely manner commensurate with their importance to

safety and risk based on the following:

initial problem identification, characterization, and tracking;

disposition of operability/reportability issues;

evaluation of safety significance/risk and priority for resolution;

identification of repetitive problems;

identification of contributing causes;

identification and implementation of effective corrective actions;

Enclosure

28

resolution of NCVs tracked in the corrective action system; and

implementation/consideration of risk-significant operational experience feedback.

These activities represented one inspection sample.

b.

Findings

No findings of significance were identified.

.3

Job-In-Progress Reviews

a.

Inspection Scope

The inspectors observed the following three jobs that were being performed in radiation

areas, airborne radioactivity areas, or high radiation areas for observation of work

activities that presented the greatest radiological risk to workers:

Drywell Cooler Number Four Removal;

Cutout and Replace Check Valve E1100F031A; and

Perform Refuel Activities.

The inspectors reviewed radiological job requirements for the three activities including

RWP requirements and work procedure requirements, and attended As-Low-As-Is-

Reasonably-Achievable (ALARA) job briefings.

These activities represented one inspection sample.

Job performance was observed with respect to these requirements to verify radiological

conditions in the work area were adequately communicated to workers through pre-job

briefings and postings. The inspectors also verified the adequacy of radiological

controls including required radiation, contamination, and airborne surveys for system

breaches; radiation protection job coverage which included audio and visual surveillance

for remote job coverage; and contamination controls.

These activities represented one inspection sample.

b.

Findings

No findings of significance were identified.

.4

Radiation Worker Performance

a.

Inspection Scope

During job performance observations, the inspectors evaluated radiation worker

performance with respect to stated radiation protection work requirements and

evaluated whether workers were aware of the significant radiological conditions in their

workplace, the RWP controls and limits in place, and that their performance had

accounted for the level of radiological hazards present.

Enclosure

29

These activities represented one inspection sample.

The inspectors reviewed radiological problem reports which found the cause of the

event was due to radiation worker errors to determine if there was an observable pattern

traceable to a similar cause, and to determine if this perspective matched the corrective

action approach taken by the licensee to resolve the reported problems. These

problems, along with planned and taken corrective actions were discussed with the

Radiation Protection Manager.

These activities represented one inspection sample.

b.

Findings

No findings of significance were identified.

.5

Radiation Protection Technician (RPT) Proficiency

a.

Inspection Scope

During job performance observations, the inspectors evaluated RPT performance with

respect to radiation protection work requirements and evaluated whether they were

aware of the radiological conditions in their workplace, the RWP controls and limits in

place, and if their performance was consistent with their training and qualifications with

respect to the radiological hazards and work activities.

These activities represented one inspection sample.

The inspectors reviewed two radiological problem reports which found the cause of the

event was radiation protection technician error to determine if there was an observable

pattern traceable to a similar cause, and to determine if this perspective matched the

corrective action approach taken by the licensee to resolve the reported problems.

These activities represented one inspection sample.

b.

Findings

No findings of significance were identified.

2OS2 As-Low-As-Is-Reasonably-Achievable Planning And Controls (ALARA) (IP 71121.02)

.1

Inspection Planning

a.

Inspection Scope

The inspectors reviewed plant collective exposure history, current exposure trends,

ongoing and planned activities in order to assess current performance and exposure

challenges. This included determining the plants current 3-year rolling average for

collective exposure in order to help establish resource allocations and to provide a

perspective of significance for any resulting inspection finding assessment.

Enclosure

30

These activities represented one inspection sample.

The inspectors reviewed the outage work scheduled during the inspection period and

associated work activity exposure estimates for the following five work activities which

were likely to result in the highest personnel collective exposures:

Drywell Cooler Number Four Removal;

Cutout and Replace Check Valve E1100F031A;

Refuel Floor Activities;

Main Steam Reheater Replacement; and

In-Service Inspections.

These activities represented one inspection sample.

The inspectors determined site specific trends in collective exposures and source-term

measurements. The inspectors reviewed procedures associated with maintaining

occupational exposures ALARA and processes used to estimate and track work activity

specific exposures.

These activities represented two inspection samples.

b.

Findings

No findings of significance were identified.

.2

Radiological Work Planning

a.

Inspection Scope

The inspectors evaluated the licensees list of planned work activities for RF11 ranked

by estimated exposure that were in progress and reviewed the following three work

activities of exposure significance:

06-1113, CRD Exchange;

06-1205, East/West MSR Replacement; and

06-1124, Drywell Cooler Number Four Removal.

For these three activities, the inspectors reviewed the ALARA work activity evaluations,

exposure estimates, and exposure mitigation requirements in order to verify the licensee

had established procedures and engineering and work controls that were based on

sound radiation protection principles in order to achieve occupational exposures that

were ALARA. This also involved determining that the licensee had reasonably grouped

the radiological work into work activities, based on historical precedence, industry

norms, and/or special circumstances.

The inspectors compared the results achieved including dose rate reductions and

person-rem used with the intended dose established in the licensees ALARA planning

for these three work activities. Reasons for inconsistencies between intended and

actual work activity doses were reviewed.

Enclosure

31

These activities represented one inspection sample.

b.

Findings

No findings of significance were identified.

.3

Verification of Dose Estimates and Exposure Tracking Systems

a.

Inspection Scope

The licensees process for adjusting exposure estimates or re-planning work, when

unexpected changes in scope, emergent work or higher than anticipated radiation levels

were encountered, was evaluated. This included determining that adjustments to

estimated exposure (intended dose) were based on sound radiation protection and

ALARA principles and not adjusted to account for failures to control the work. The

frequency of these adjustments was reviewed to evaluate the adequacy of the original

ALARA planning process.

These activities represented one inspection sample.

b.

Findings

No findings of significance were identified.

.4

Job Site Inspections and ALARA Control

a.

Inspection Scope

The inspectors observed the following five jobs that were being performed in radiation

areas, airborne radioactivity areas, or high radiation areas for observation of work

activities that presented the greatest radiological risk to workers.

Drywell Cooler Number Four Removal;

Cutout and Replace Check Valve E1100F031A;

Refuel Floor Activities;

Main Steam Reheater Replacement; and

In-Service Inspections.

The licensees use of engineering controls to achieve dose reductions was evaluated to

verify procedures and controls were consistent with the licensees ALARA reviews,

sufficient shielding of radiation sources was provided for, and the dose expended to

install/remove the shielding did not exceed the dose reduction benefits afforded by the

shielding.

These activities represented one inspection sample.

b.

Findings

No findings of significance were identified.

Enclosure

32

.5

Radiation Worker Performance

a.

Inspection Scope

Radiation worker and RPT performance was observed during work activities being

performed in radiation areas, airborne radioactivity areas, and high radiation areas that

presented the greatest radiological risk to workers. The inspectors evaluated whether

workers demonstrated the ALARA philosophy in practice by being familiar with the work

activity scope and tools to be used, by utilizing ALARA low dose waiting areas, and that

work activity controls were being complied with. Also, radiation worker training and skill

levels were reviewed to determine if they were sufficient relative to the radiological

hazards and the work involved.

These activities represented one inspection sample.

b.

Findings

No findings of significance were identified.

4.

OTHER ACTIVITIES (OA)

4OA2 Identification and Resolution of Problems (71152)

.1

Routine Review of Identification and Resolution of Problems

a.

Inspection Scope

As discussed in previous sections of this report, the inspectors routinely reviewed issues

during baseline inspection activities and plant status reviews to verify they were being

entered into the licensee's corrective action system at an appropriate threshold,

adequate attention was being given to timely corrective actions, and adverse trends

were identified and addressed.

b.

Findings

No findings of significance were identified.

.2

Semi-Annual Trend Review

a.

Inspection Scope

The inspectors performed a screening review of each item entered into the licensees

corrective action program to identify trends that might indicate the existence of a more

significant safety issue. The inspectors considered repetitive or closely related issues

that may have been documented by the licensee outside the normal corrective action

program, such as in:

C

trend reports or performance indicators,

C

major equipment problem lists,

Enclosure

33

C

repetitive and/or rework maintenance lists,

C

departmental problem/challenges lists,

C

system health reports,

C

quality assurance audit/surveillance reports,

C

self assessment reports,

C

maintenance rule assessments, or

C

corrective action backlog lists.

The inspectors verified the licensee was identifying issues at an appropriate threshold

and entering them into their corrective action program by comparing those issues

identified by the NRC during the conduct of the plant status and inspectable area

portions of the program with those issues identified by the licensee.

b.

Issues

Unidentified drywell leakage was fluctuating after startup from RF11 but has since

leveled out. From the lowest value, unidentified leakage has increased from about

0.06 gpm to an average daily value of 0.14 gpm. Additionally, the inner seal pressure

for the B reactor recirculation pump has been fluctuating by as much as 40-60 psig;

however, there does not appear to be a correlation between the seal pressure

oscillations and drywell leakage. These issues are in the licensees corrective action

program as CARDs 06-24313 for the unidentified leakage and 06-23791 for the seal

pressure oscillations.

4OA3 Event Followup (71153)

.1

Reactor Scram due to Main Transformer Fault

a.

Inspection Scope

As described in Section 1R20.3 of this report, the inspectors responded to the control

room on June 15, 2006, when the reactor automatically shut down as a result of the

failure of main unit transformer 2B. The inspectors observed plant parameters and

status, evaluated the performance of mitigating systems and licensee actions, confirmed

that the licensee properly classified the event in accordance with emergency action level

procedures and made timely notifications to NRC and state/county governments, as

required by 10 CFR 50.72 (Event Number 42643). The inspectors determined and

communicated details regarding the event to NRC management, risk analysts and

others in Region III and Headquarters as input to an evaluation per Management

Directive 8.3 for determining the appropriate level of event response. Based on the

events that occurred, routine resident inspection efforts were deemed appropriate.

b.

Findings

No findings of significance were identified.

Enclosure

34

.2

Review of Licensee Event Reports (LER)

a.

(Closed) LER 50-341/2006-001: At 0039 hours4.513889e-4 days <br />0.0108 hours <br />6.448413e-5 weeks <br />1.48395e-5 months <br /> on April 1, 2006, Fermi 2 feedwater line

check valves B2100F010A and B2100F076A failed their LLRT. The air leakage rate of

the inboard check valve B2100F010A was 324.21 standard cubic feet per hour (SCFH),

and the leakage rate of outboard check valve B2100F076A was above the

measurement capability of the leak rate monitor. The penetration (X-9A) minimum-

pathway air leakage value was determined to be 324.21 SCFH which is greater than the

allowable containment leakage rate (La) value of 296.3 SCFH per TS 5.5.12 and higher

than the allowable secondary containment bypass leakage rate of 0.1 La or 29.63 SCFH

per TS Surveillance Requirement 3.6.1.3.11. The B2100F076A failure was attributed to

soft seat degradation which was primarily caused by extending its service time to three

operating cycles. The B2100F010A valve failure was attributed to soft seat degradation

due to a slight misalignment of the valve disc to the in-body seat, compounded by wear

between the internal shaft and valve disc. The slight misalignment caused the soft seat

along the top portion of the disc to contact the seat first, resulting in a scraping action as

the disc flexed to its full seat position. For both valves, the soft seats were replaced,

and the soft seat service time has been limited to two operating cycles. The internal

shaft for the B2100F010A valve was replaced, and the alignment between the disc and

the valve seat was adjusted. Both valves were retested and met their associated LLRT

acceptance criteria prior to restart of the unit.

The LER was reviewed by the inspectors. No findings of significance were identified

and no violation of NRC requirements occurred. The licensee documented the LLRT

failure in CARD 06-21751. This LER is closed.

4OA6 Exit Meetings

.1

Exit Meeting Summary

On July 11, 2006, the inspectors presented the inspection results to Mr. D. Cobb and

other members of licensee management at the conclusion of the inspection. The

inspectors asked the licensee whether any material examined during the inspection

should be considered proprietary. No proprietary information was identified.

.2

Interim Exit Meetings

On April 7, 2006, an interim exit meeting was conducted for the Access Control to

Radiological Areas and ALARA inspection with Mr. Kevin Hlavaty, Plant Manager, and

other licensee staff.

4OA7 Licensee-Identified Violations

The following violation of very low significance was identified by the licensee and is a

violation of NRC requirements, which meet the criteria of Section VI of the NRC

Enforcement Manual, NUREG-1600, for being dispositioned as an NCV.

Enclosure

35

Cornerstone: Public Radiation Safety

The licensees procedure 67.000.103, Surveying of Outgoing Shipments, directs the

staff to survey outgoing vehicles used to carry an exclusive use shipment of radioactive

material. The procedure relies on the proper identification of the incoming shipment as

an exclusive use shipment. This procedure is used to implement the requirements of

49 CFR 173.443 and 49 CFR 177.843 that require the specific release survey of

vehicles in exclusive use situations. Contrary to the above, and as described in

CARD 06-21389, on March 20, 2006, an exclusive use radioactive material shipment

was received by the licensee. The shipment contained one package of Limited Quantity

radioactive material and four boxes of non-radioactive material and the radiation

protection staff assigned to accept the shipment incorrectly identified the shipment as a

non-exclusive use shipment. After the packages were removed from the conveyance,

the vehicle was released without the required survey. This was identified by licensee

supervision but not before the vehicle had departed the site. The carrier was contacted

and the vehicle returned to the licensees site before further transportation activity had

commenced and a survey was completed. No contamination was found and no dose

rates above background were identified. The finding is of very low safety significance

because it did not result in an unmonitored release nor were any dose limits

approached.

ATTACHMENT: SUPPLEMENTAL INFORMATION

Attachment

1

KEY POINTS OF CONTACT

Licensee

D. Gipson, Chief Nuclear Officer

D. Cobb, Assistant Vice President, Nuclear Generation

K. Hlavaty, Plant Manager

S. Bartman, Nuclear Production

J. Davis, Manager, Outage Management

R. Gaston, Licensing Manager

S. Hassoun, Principal Engineer, Licensing

H. Higgins, Radiation Protection Manager

J. Korte, Manager, Nuclear Security

J. Plona, Engineering Director

NRC

C. Lipa, Chief, Division of Reactor Projects, Branch 4

Attachment

2

LIST OF ITEMS OPENED, CLOSED, AND DISCUSSED

Opened

05000341/2006003-05

URI

Inappropriate Use of Risk in Operability Evaluations

(Section 1R15.3)

Opened and Closed

05000341/2006003-01

NCV

Unauthorized Transient Combustibles in Safety-Related

Areas (Section 1R05.2)05000341/2006003-02

NCV

Improper Storage of Chemicals Affecting Fire Fighting

Response (Section 1R05.3)05000341/2006003-03

NCV

Inadequate Maintenance Risk Assessment

(Section 1R13.2)05000341/2006003-04

NCV

Improper Evaluation of Standby Liquid Control Operability

During Tank Sparging (Section 1R15.2)05000341/2006003-06

NCV

Inadequate Controls for Venting the Reactor Pressure

Vessel Head (Section 1R20.1)

Closed

05000341/2006-001 LER

Excessive Feedwater Check Valve Leakage at Containment

Penetration

Discussed

None.

Attachment

3

LIST OF DOCUMENTS REVIEWED

The following is a list of documents reviewed during the inspection. Inclusion on this list does

not imply that the NRC inspectors reviewed the documents in their entirety but rather that

selected sections of portions of the documents were evaluated as part of the overall inspection

effort. Inclusion of a document on this list does not imply NRC acceptance of the document or

any part of it, unless this is stated in the body of the inspection report.

1R01: Adverse Weather Protection

CARD 06-23861, 06/05/06; Procedure Enhancement for TBHVAC (NRC Comment)

Procedure 27.000.06, Rev 0, 02/27/03; Performance Evaluation Procedure, Hot Weather

Operations

Open/Closed Work Requests by Related Work Code; 05/04/06

1R04: Equipment Alignment

Drawing 6M721-5706-3, 2/16/00; RHR Service Water Make Up Decant and Overflow Systems

Functional Operating Sketch

Drawing 6M721-5706-1, 3/5/04; Residual Heat Removal (RHR) Division II Functional Operating

Sketch

03-00120, 01/02/03; Pinhole leak in piping

03-13694, 6/17/03; Document the Condition of General Service Water Piping

04-24918, 10/25/04; P4100F402A installed at the bottom of the pipe

06-11615, 05/19/06; EDG Electrical Lineup Load Description Changes

06-21618, 03/28/06; E1100F050A Failed PI Leak Test SR 3.4.5.1

06-22730, 4/24/06; NRC-Identified Concerns in GSW Pumphouse

06-23447, 05/18/06; 23.205 Att 1B enhancement

06-23494, 05/20/06; E1100F050A actuator failed to open valve

23.131, Rev.86; General Service Water System

43.000.005, Rev. 30; Visual Examination of Piping and Components (VT-2)

23.208, Rev. 81; RHR Complex Service Water Systems

23.205, Rev. 94; Residual Heat Removal System

1R05: Fire Protection

CARD 06-23365; Door is not latching; Dated May 15, 2006 (NRC-Identified)

CARD 06-23388; Transient Combustibles in the RHR; Dated May 16, 2006 (NRC-Identified)

MOP11; Fire Protection; Revision 10

Fire Brigade Drill Scenario 6, Rev. 11/29/94; First Floor Radioactive Waste Chemical Lab

Storage Area

Fire protection Pre-Plan FP-RDWST, Rev. 4; Radwaste Building Zones 22, 23, 24, and 25

1R06: Flood Protection Measures

CARD 06-21354; High Pressure Coolant Injection Room Flooded due to Drains backing Up;

3/18/06

CARD 06-22600; Moderate Energy Line Break Evaluation; 4/21/06 (NRC-Identified)

Attachment

4

Nuclear Generation Memo TMPE-94-0308; May 18, 1994; Flood Protection Review

6M721-2223, Rev U, 11/24/06; Diagram Equipment Drains All Floors Auxiliary and Reactor

Buildings

6M721-2224, Rev W, 11/24/04; Diagram Floor Drains All Floors Auxiliary and Reactor Buildings

6M721-2032, Rev BO, 04/19/06; Sump Pump Diagram Radwaste System

6M721-2032-1, Rev AI, 04/19/06; Sump Pump Diagram Radwaste System

1R07: Heat Sink Performance

WR TG25060421; Perform RHR Division II Heat Exchanger Performance Test; 3/22/06

1R11: Licensed Operator Requalification

Scenario SS-OP-802-3300, Rev. 0; Anticipated Transient Without Scram with Small Steam

Leak; 1/26/06

1R12: Maintenance Effectiveness

Design Specification 3071-128-EZ-06; Electrical Design Instructions Molded Case Circuit

Breakers

Maintenance Rule Conduct Manual MMR, Appendix E, Rev 4; Maintenance Rule SSC Specific

Functions

Memo dtd 01/30/06, TMIS-06-0011; Summary of Expert Panel Meeting 184 Conducted

January 24, 2006

CTG11-1 Get Well Plan; July 2003

Deviation Event Report 93-0528, 09/15/93

Vendor Manual VME5-18, Rev 0; Spectrum Technologies, Series 5600, MCC

CARD 97-10182, 10/27/97; Defective Molded Case Circuit Breaker

CARD 03-01098,05/30/03; Reactor Protection System - Function Failure

03-19510,07/20/03; Safety Eval 95-0002 is Used as an Operability Evaluation for LPCI with the

RHR Minimum Flow Valves Open

CARD 04-22685, 07/02/04; Generator Transformer - Function Failure

CARD 04-23307. 08/03/04; Motor Control Centers & Dist. Cabinets

CARD 05-23490, 06/21/05; Auxiliary Electrical - Function Failure

CARD 06-21363, 04-02-06; Auxiliary Electrical - Function Failure

CARD 06-21527, 04/09/06; Residual Heat Removal System - Function Failure

CARD 06-22270, 04/12/06, Maintenance Rule Function T4100-09 should be included in

Maintenance Rule Scope Investigation

Procedure 35.306.008, Rev 46; Maintenance Procedure, ITE Gould Motor Control Center Load

Compartment

Procedure 35.306.018, Rev 5; Maintenance Procedure, Spectrum Technology Motor Control

Center Load Compartment

1R13: Maintenance Risk Assessment and Emergent Work Evaluation

Fermi 2 Daily Plant Status, April 2, 2006

Schedulers Evaluation for Fermi 2, April 2, 2006

Fermi 2 Daily Plant Status, April 17, 2006

Schedulers Evaluation for Fermi 2, April 17, 2006

Attachment

5

Fermi 2 Daily Plant Status, April 30, 2006

Schedulers Evaluation for Fermi 2, April 30, 2006

Fermi 2 Daily Plant Status, June 26, 2006

Schedulers Evaluation for Fermi 2, June 26, 2006

CARD 06-21892, 4/4/06; NRC Questions related to Temporary Cooling Installed for Division I

Battery Test (NRC-Identified)

CARD 06-24495, 7/7/06; Work Risk Assessment and Temporary Equipment Controls

(NRC-Identified)

WR 0219060414; Perform 42.309.05 Division I (5 Year) 130/260 VDC batter Check (2A-1 Only)

WR 1219060414; Perform 42.309.05 Division I (5 Year) 130/260 VDC batter Check (2A-2 Only)

1R14: Non-Routine Events

CARD 06-24113; Main Steam Bypass Valves Opened Unintentionally During Power Ascension;

6/18/06

CARD 06-23588; Mode 5 Reactor SCRAM During Installation of SRM Shorting Links; 5/24/06

CARD 06-23501; Full In Light for Control Rod 50-27 on Full Core Display is Intermittent;

5/20/06

1R15: Operability Evaluations

Drawing - 5744, Rev. BK; Emergency Equipment Cooling Water Division I; 11/23/05

WR 000Z060107; Remove and Reinstall Insulation on E1100F031B; 2/9/06

WR 000Z062027; Replace Contaminated Insulation; 6/12/06

CARD 06-24156; Affects of Accidents not Addressed in Insulation Removal Evaluation for

E1100F031B; 6/20/06 (NRC Identified)

CARD 01-17302; There are no Site Guidelines for Insulation Removal on Operable Equipment;

8/14/01

CARD 06-23898; EECW M/U Pump IST Flow Unattainable; 6/7/06

CARD 02-14782; Engineering Evaluation for On-Line Insulation Removal; 6/27/02

CARD 03-16498; Engineering Evaluation for On-Line Insulation Removal; 9/9/03

CARD 05-21940; Engineering Evaluation for On-Line Insulation Removal; 3/23/05

CARD 06-23913; Replace Contaminated Insulation; 6/8/06

CARD 06-23785; Standby Liquid Control Operability During Sparging Activities; 6/1/06 (NRC-

Identified)

CARD 99-13240; Inoperability of Standby Liquid Control During Air Sparging; 4/15/99

1R19: Post-Maintenance Testing

EDP - 31880 120 KV Switchyard Upgrade

Engineering Change Request 33690-1, Rev A, 03/14/06; Replacement of Drywell Cooler Coils

T470B003 and T4700B004

Equivalent Replacement Evaluation (ERE) 34173, Rev 0, 04/18/06; E1150F608 MOV Motor

Replacement

Oil Sample Analysis Reports for C1106C001A, E Control Rod Drive Pump; 01/01/06 -

06/29/06

CARD 06-22258, 04/12/06; CTG equipment issues discovered during IPTE 04-02

CARD 06-22982, 4/30/06; Inboard MSIV A will not slow close

CARD 06-23031, 5/1/06; MSIV B2103F028B RPS Limit Switch did not actuate when expected

Attachment

6

CARD 06-22634, 4/22/06; A Inboard MSIV limit switch, PIS B21N572A, will not change state

Drawing SD-F-0179, Rev. A, 9/25/05; Diagram Line Breaker Control 120KV, POS GK

Drawing SD-2500-01, Rev. A, 2/28/06; One Line Diagram Plant 4160V & 480V

Drawing SD-2500-02, Rev. A, 2/23/06; One Line Diagram 13.8KV

Drawing SD-F-0001, Rev. A, 2.23/06; One Line Diagram 120 KV Switchyard

IPTE 04-02, 120KV Switchyard Upgrade

Procedure 24.137.01, Rev. 34; Main Steam Isolation Channel Functional Test

24.206.01, Rev 63, 05/08/06; RCIC System Pump and Valve Operability Test

43.000.005, Rev 30, 03/22/06; Visual Examination of Piping and Components (VT-2)

43.401.303, Rev 32, 10/24/05; Local Leakage Rate Testing for Penetration X-9A

WR B203040100, 04/10/06; B2100F010A - Nuclear Boiler Feedwater Supply Inboard Primary

Containment Check Valve

WR 000Z050487, 04/29/06;B3105F031A - Reactor Recirculation Pump A Discharge Valve

WR T210040100, 04/10/06; B2100F076A - Nuclear Boiler Feedwater Supply Check Valve

WR 000Z052131, 04/19/06; Inservice Testing, Drywell Cooler #4

WR 000Z060156, 6/19/06; E Control Rod Drive Inboard Pump Bearing Oil level Bulls eye Dirty

1R20: Refueling and Outage Activities

Apparent Cause Determination for Damage Found in the Main Generator During RF11 Robot

Inspections CARD 06-21922

Inspection Requirement Form, Requisition Number: 9086929; 04/19/2006

Drawing 6M721-3722, Rev A; Flow Diagram & Details of Purging Unit - Reactor Pressure

Vessel - Unit 2

Safety Tagging Record 2006-002089

CARD 06-21534, 03/26/2006; Continuous Air Monitor Alarm on Refueling Floor

CARD 06-22590, 04/21/2006; NRC identified concern with Div 1 Core Spray and Defense in

Depth Investigation

CARD 06-22642, 04/22/2006; Are EDG Surveillances Testing What They Are Setup to Test

CARD 06-22667, 04/23/2006; RPV Venting Unit Configuration Control Discrepancies

CARD 06-23114, 05/03/2006; NRC Concern: Review of ERE-34173 E1150F608 MOV Motor

Replacement

CARD 06-23793, 06/02/2006; NRC Concern - Material Released Without the Requirements of

EED Being Verified

Procedure 24.106.06, Rev 25; Surveillance Procedure, SCRAM Discharge Volume Vent and

Drain Valves SCRAM Operability Test

Procedure 32.000.07, Rev 33; Crane Operation Procedure, Reactor Building Crane Operation

Procedure 35.717.001, Rev 29; Maintenance Procedure, Reactor Building Crane - Quarterly

Preventive Maintenance

Procedure 35.717.003, Rev 3; Maintenance Procedure, Reactor Building Crane - Annual PM

Inspection

Procedure 43.401.303, Rev 32; Surveillance Procedure, Local Leakage Rate Testing for

Penetration X-9A

Work Control Conduct Manual MWC13, Rev 0; Outage Nuclear Safety

Maintenance Conduct Manual MMA07, Rev 14; Hoisting, Rigging and Load Handling

Attachment

7

1R22: Surveillance Testing

Drawing 6M721-5703-1, Rev. Y; Control Rod Drive System Functional Operating Sketch

CARD 06-22739, 4/24/06; Acrid smell from EDG #13 local control cabinet

CARD 06-23031, 5/1/06; MSIV B2103F028B RPS Limit Switch did not actuate when expected

CARD 06-22653, 04/23/06; HCU 46-27 Conduit for wiring to accumulator pressure switch

needs repair

CARD 06-22999, 05/01/06; Enhancements to 24.405.03

CARD 06-21681; Potential Enhancement for MSIV Switch Calibrations; 3/20/06 (NRC-

Identified)

CARD 06-21720; NRC Question Regarding MSIV Switch Testing; 3/31/06 (NRC-Identified)

CARD 06-22046; Loss of SLC Squib Valve A Continuity Light During Performance of

24.139.03; 4/7/06

Procedure 24.106.06, Rev 25; Surveillance Procedure, SCRAM Discharge Volume Vent and

Drain Valves SCRAM Operability Test

Procedure 24.106.08, Rev. 3; CRD Hydraulic Unit Accumulator Integrity Test

Procedure 24.137.01, Rev. 34; Main Steam Isolation Channel Functional Test

Procedure 24.405.03, Rev. 33; Secondary Containment Operability Test

Procedure 24.307.03, Rev. 38; EDG 13 - Loss of Offsite Power and ECCS Start with Loss of

Offsite Power Test

Procedure 24.202.02, Rev. 42; HPCI Flow Rate Test at 165 psig Reactor Steam Pressure

Procedure 24.206.04, Rev. 44; RCIC System Automatic Actuation and Flow Test

Procedure 43.401.500, Rev 34; Surveillance Procedure, Local Leakage Rate Testing for

Penetration X-7A, X-7B, X-7C, and X-7D

Procedure 43.401.500, Rev 35; Surveillance Procedure, Local Leakage Rate Testing for

Penetration X-7A, X-7B, X-7C, and X-7D

Procedure 24.402.06; Rev. 32; Drywell to Suppression Chamber Bypass Leak Test

Procedure 35.139.002; Rev. 27; SLC System Explosive Valve Insert Replacement

Procedure 24.139.03, Rev. 40; SLC Manual Initiation, RWCU Isolation, and Storage tank

Heater Operability Test

WR 0311060425; Perform 24.402.06 Drywell to Suppression Chamber Bypass Leak Test;

3/25/06

WR 0518041022; Perform 44.010.063 RPS MSIV Outboard Valve Limit Switch, Div. I and II,

Calibration

WR 1245060421; Perform 24.139.03 SLC Loop B Pump Flow, Manual Initiate, and Squib

Firing; 4/21/06

1EP6: Drill Evaluation

Scenario SS-OP-802-3300, Rev. 0; Anticipated Transient Without Scram with Small Steam

Leak; 1/26/06

2OS1: Access Control to Radiologically Significant Areas

CARD 05-26818; Primary Containment Atmosphere Sample Pump; T5001-C003 Will Not Start;

dated December 5, 2005

CARD 06-11546; WGI Employee Felt Something in His Left Eye after Removing Protective

Clothing at Drywell Step-off Pad; dated April 5, 2006

CARD 06-21534; High Radiation Alarm on Refuel Floor; dated March 26, 2006

Attachment

8

CARD 06-21640; Unnecessary Contamination of Personnel; dated March 29, 2006

CARD 06-21639; Evaluate Dose an Dose Rate Alarms for Fast Entry Electronic Dosimeters;

dated March 29, 2006

CARD 06-20962; Worker Electronic Dosimeter Alarm on Incorrect Task; dated February 23,

2006

CARD 06-21177; Unexpected Dose Rate Alarm; dated March 8, 2006

CARD 06-21787; Entering High Radiation Area on Incorrect Task; dated April 1, 2006

CARD 06-21807; Evaluate Reactor Building Ventilation Impact on the Spread of Contamination

during RF11 Vessel Fill Up; dated April 2, 2006

CARD 06-21857; Drywell Stepoff Pad Poor Radiation Protection Practices; dated April 3, 2006

CARD 06-21873; Potential Release of Radioactive Contamination; dated April 4, 2006

CARD 06- 21868; Workers Entered Top of Torus High Radiation Area on Wrong Radiation

Work Permit; dated April 4, 2006

CARD 06-21944; Foreign Material Found Inside Main Condenser Upper Steam Space; dated

April 5, 2006

CARD 06-21958; Worker Received Puncture Wound; dated April 6, 2006

EP-225; Radiological Medical Emergencies; Revision 13

RF11 ALARA Self-Assessment; dated April 4, 2006

2OS2 As-Low-As-Is-Reasonably-Achievable Planning And Controls (ALARA)

RWP 06-1110; In-Service Inspections; Revision 0

RWP 06-1103; Install and Remove Temporary Shielding, Install Permanent Shielding;

Revision 0

RWP 06-1105; Job Progress for Scaffold Activities in the Reactor Building Steam Tunnel and

Drywell; Revision 0

RWP 06-1124; Replace Number 4 Drywell Cooler; Revision 4

RWP 06-1164; E1100F031A Cutout and Replace Check Valve; Revision 0

RWP 06-1251; Perform Refuel Activities on Reactor Building 5; Revision 0

CARD 06-21765; Work Initiated Without Radiation Protection Review; dated April 1, 2006

CARD 06-21911; E100F031A Glovebag Not Installed Properly; dated April 5, 2006

CARD 06-21947; E1100F060A Re-pack Extra Time and Dose Above Initial Estimate; dated

April 5, 2006

Procedure 63.000.100; Respirator Evaluation Work Sheet (RWP 06-1117); Revision 0

4OA2: Identification and Resolution of Problems

CARDs initiated between 1/1/06 and 06/30/06

4OA3: Event Followup (71153)

NRC-06-0037 Letter; Licensee Event report No. 2006-001, Excessive Feedwater Check Valve

Leakage At Containment Penetration; dated May 24, 2006

4OA7 Licensee-Identified Violations

CARD 06-21389; Failure to Perform Required Surveys in Accordance with

Procedure 67.000.102; dated March 21, 2006

Procedure 67.000.103; Survey of Outgoing Radioactive Material Shipments; Revision 16

Procedure 67.000.102; Survey of Incoming Radioactive Material Shipments; Revision 0

Attachment

9

LIST OF ACRONYMS USED

ALARA

As Low As Reasonable Achievable

CARD

Condition Assessment Resolution Document

CDF

Core Damage Frequency

CFR

Code of Federal Regulations

CTG

Combustion Turbine Generator

DRP

Division of Reactor Projects

EDG

Emergency Diesel Generator

GSW

General Service Water

HPCI

High Pressure Coolant Injection

IMC

Inspection Manual Chapter

LER

Licensee Event Report

LERF

Large Early Release Frequency

LLRT

Local Leak Rate Test

MCC

Motor Control Center

MSIV

Main Steam Isolation Valve

NCV

Non-Cited Violation

NRC

Nuclear Regulatory Commission

PI

Performance Indicator

PMT

Post-Maintenance Testing

RCIC

Reactor Core Isolation Cooling

RCS

Reactor Coolant System

RHR

Residual Heat Removal

RHRSW

Residual Heat Removal Service Water

RPS

Reactor Protection System

RPSMG

Reactor Protection System Motor Generator

RPT

Radiation Protection Technician

RWCU

Reactor Water Cleanup

RWP

Radiation Work Package

SCFH

Standard Cubic Feet Per Hour

SCFM

Standard Cubic Feet Per Minute

SDP

Significance Determination Process

SGTS

Standby Gas Treatment System

SLC

Standby Liquid Control

SPAR

Standardized Plant Analysis Risk

SRA

Senior Reactor Analyst

TM

Temporary Modifications

TS

Technical Specifications

UFSAR

Updated Final Safety Analysis Report

WR

Work Request