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{{#Wiki_filter:August 2, 2006Mr. Donald K. CobbAssistant Vice President
{{#Wiki_filter:August 2, 2006
Mr. Donald K. Cobb
Assistant Vice President
Nuclear Generation
Nuclear Generation
Detroit Edison Company
Detroit Edison Company
6400 North Dixie Highway
6400 North Dixie Highway
Newport, MI 48166SUBJECT:FERMI POWER PLANT, UNIT 2, NRC INTEGRATED INSPECTION REPORT 05000341/2006003Dear Mr. Cobb:
Newport, MI 48166
On June 30, 2006, the U.S. Nuclear Regulatory Commission (NRC) completed an integratedinspection at your Fermi Power Plant, Unit 2. The enclosed report documents the inspection
SUBJECT:         FERMI POWER PLANT, UNIT 2, NRC INTEGRATED
findings which were discussed on July 11, 2006, with you and other members of your staff.The inspection examined activities conducted under your license as they relate to safety and tocompliance with the Commission's rules and regulations and with the conditions of your license.  
                INSPECTION REPORT 05000341/2006003
Dear Mr. Cobb:
On June 30, 2006, the U.S. Nuclear Regulatory Commission (NRC) completed an integrated
inspection at your Fermi Power Plant, Unit 2. The enclosed report documents the inspection
findings which were discussed on July 11, 2006, with you and other members of your staff.
The inspection examined activities conducted under your license as they relate to safety and to
compliance with the Commissions rules and regulations and with the conditions of your license.
The inspectors reviewed selected procedures and records, observed activities, and interviewed
The inspectors reviewed selected procedures and records, observed activities, and interviewed
personnel.Based on the results of this inspection, five findings of very low safety significance wereidentified, all of which involved violations of  
personnel.
NRC requirements. However, because thesefindings were of very low safety significance and because the issues were entered into your
Based on the results of this inspection, five findings of very low safety significance were
corrective program, the NRC is treating these findings as Non-Cited Violations in accordancewith Section VI.A.1 of the NRC's Enforcement Policy. If you contest the subject or severity of
identified, all of which involved violations of NRC requirements. However, because these
findings were of very low safety significance and because the issues were entered into your
corrective program, the NRC is treating these findings as Non-Cited Violations in accordance
with Section VI.A.1 of the NRCs Enforcement Policy. If you contest the subject or severity of
a Non-Cited Violation, you should provide a response within 30 days of the date of this
a Non-Cited Violation, you should provide a response within 30 days of the date of this
inspection report, with the basis for your denial, to the U.S. Nuclear Regulatory Commission,
inspection report, with the basis for your denial, to the U.S. Nuclear Regulatory Commission,
ATTN: Document Control Desk, Washington, DC 20555-0001, with a copy to the Regional
ATTN: Document Control Desk, Washington, DC 20555-0001, with a copy to the Regional
Administrator, U.S. Nuclear Regulatory Commission - Region III, 2443 Warrenville R oad,Suite 210, Lisle, IL 60532-4352; the Director, Office of Enforcement, U.S. Nuclear RegulatoryCommission, Washington, DC 20555-0001; and the Resident Inspector Office at the
Administrator, U.S. Nuclear Regulatory Commission - Region III, 2443 Warrenville Road,
Fermi 2facility.In accordance with 10 CFR 2.390 of the NRC's "Rules of Practice," a copy of this letter andits enclosure will be made available electronically for public inspection in the NRC Public
Suite 210, Lisle, IL 60532-4352; the Director, Office of Enforcement, U.S. Nuclear Regulatory
D. Cobb-2-Document Room or from the Publicly Available Records (PARS) component of  
Commission, Washington, DC 20555-0001; and the Resident Inspector Office at the Fermi 2
NRC'sdocument system (ADAMS). ADAMS is accessible from the NRC Web site at
facility.
http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room).Sincerely,/RA/Christine A. Lipa, ChiefBranch 4
In accordance with 10 CFR 2.390 of the NRCs Rules of Practice, a copy of this letter and
Division of Reactor ProjectsDocket No. 50-341License No. NPF-43Enclosure:Inspection Report 05000341/2006003 w/Attachment: Supplemental Informationcc w/encl:K. Hlavaty, Plant ManagerR. Gaston, Manager, Nuclear Licensing
its enclosure will be made available electronically for public inspection in the NRC Public
D. Pettinari, Legal Department
 
Michigan Department of Environmental Quality
D. Cobb                                         -2-
  Waste and Hazardous Materials Division
Document Room or from the Publicly Available Records (PARS) component of NRCs
M. Yudasz, Jr., Director, Monroe County
document system (ADAMS). ADAMS is accessible from the NRC Web site at
  Emergency Management Division
http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room).
Supervisor - Electric Operators
                                            Sincerely,
State Liaison Officer, State of Michigan
                                            /RA/
Wayne County Emergency Management Division  
                                            Christine A. Lipa, Chief
D. Cobb-2-Document Room or from the Publicly Available Records (PARS) component of  
                                            Branch 4
NRC'sdocument system (ADAMS). ADAMS is accessible from the NRC Web site at
                                            Division of Reactor Projects
http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room).Sincerely,Christine A. Lipa, ChiefBranch 4
Docket No. 50-341
Division of Reactor ProjectsDocket No. 50-341License No. NPF-43Enclosure:Inspection Report 05000341/2006003 w/Attachment: Supplemental Informationcc w/encl:K. Hlavaty, Plant ManagerR. Gaston, Manager, Nuclear Licensing
License No. NPF-43
D. Pettinari, Legal Department
Enclosure:     Inspection Report 05000341/2006003
Michigan Department of Environmental Quality
                w/Attachment: Supplemental Information
  Waste and Hazardous Materials Division
cc w/encl:     K. Hlavaty, Plant Manager
M. Yudasz, Jr., Director, Monroe County
              R. Gaston, Manager, Nuclear Licensing
  Emergency Management Division
              D. Pettinari, Legal Department
Supervisor - Electric Operators
              Michigan Department of Environmental Quality
State Liaison Officer, State of Michigan
                Waste and Hazardous Materials Division
Wayne County Emergency Management DivisionDOCUMENT NAME:E:\Filenet\ML062160540.wpd
              M. Yudasz, Jr., Director, Monroe County
G Publicly Available
                Emergency Management Division
G Non-Publicly Available
              Supervisor - Electric Operators
G Sensitive
              State Liaison Officer, State of Michigan
G Non-SensitiveTo receive a copy of this document, indicate in the concurrence box "C" = Copy without attach/encl "E" = Copy with attach/encl "N" = No copyOFFICERIIIRIIINAMERLerch:dtpCLipaDATE08/02/0608/02/06OFFICIAL RECORD COPY  
              Wayne County Emergency Management Division
Donald K. Cobb-3-ADAMS Distribution
 
:LXR1
D. Cobb                                                                       -2-
DHJ
Document Room or from the Publicly Available Records (PARS) component of NRCs
document system (ADAMS). ADAMS is accessible from the NRC Web site at
http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room).
                                                                          Sincerely,
                                                                          Christine A. Lipa, Chief
                                                                          Branch 4
                                                                          Division of Reactor Projects
Docket No. 50-341
License No. NPF-43
Enclosure:               Inspection Report 05000341/2006003
                            w/Attachment: Supplemental Information
cc w/encl:               K. Hlavaty, Plant Manager
                          R. Gaston, Manager, Nuclear Licensing
                          D. Pettinari, Legal Department
                          Michigan Department of Environmental Quality
                            Waste and Hazardous Materials Division
                          M. Yudasz, Jr., Director, Monroe County
                            Emergency Management Division
                          Supervisor - Electric Operators
                          State Liaison Officer, State of Michigan
                          Wayne County Emergency Management Division
DOCUMENT NAME:E:\Filenet\ML062160540.wpd
G Publicly Available                       G Non-Publicly Available                   G Sensitive             G Non-Sensitive
To receive a copy of this document, indicate in the concurrence box "C" = Copy without attach/encl "E" = Copy with attach/encl "N" = No copy
OFFICE              RIII                                RIII
NAME                RLerch:dtp                          CLipa
DATE                08/02/06                            08/02/06
                                                          OFFICIAL RECORD COPY
 
Donald K. Cobb                               -3-
ADAMS Distribution:
LXR1
DHJ
RidsNrrDirsIrib
RidsNrrDirsIrib
GEG
GEG
KGO
KGO
RMM3
RMM3
CAA1
CAA1
LSL (electronic IR's only)
LSL (electronic IRs only)
C. Pederson, DRS (hard copy - IR's only)
C. Pederson, DRS (hard copy - IRs only)
DRPIII
DRPIII
DRSIII
DRSIII
PLB1
PLB1
TXN
TXN
ROPreports@nrc.gov (inspection reports, final SDP letters, any letter with an IR number)  
ROPreports@nrc.gov (inspection reports, final SDP letters, any letter with an IR number)
EnclosureU. S. NUCLEAR REGULATORY COMMISSIONREGION IIIDocket No:50-341License No:NPF-43Report No:05000341/2006003
 
Licensee:Detroit Edison Company
          U. S. NUCLEAR REGULATORY COMMISSION
Facility:Fermi Power Plant, Unit 2
                          REGION III
Location:Newport, Michigan
Docket No:           50-341
Dates:April 1 through June 30, 2006
License No:         NPF-43
Inspectors:R. Michael Morris, Senior Resident InspectorT. Steadham, Resident Inspector
Report No:           05000341/2006003
A. Wilson, NRC HeadquartersM. Franke, Senior Resident Inspector, Perry
Licensee:           Detroit Edison Company
M. Jordan, NRC ConsultantR. Langstaff, Senior Reactor Inspector
Facility:           Fermi Power Plant, Unit 2
M. Mitchell, Radiation SpecialistApproved by:C. Lipa, ChiefBranch 4
Location:           Newport, Michigan
Division of Reactor Projects  
Dates:               April 1 through June 30, 2006
Enclosure 2SUMMARY OF FINDINGSIR 05000341/2006003; 04/01/2006-06/30/2006; Fermi Power Plant, Unit 2; Fire Protection,Maintenance Risk Assessment, Operability Evaluations, Refueling and Outage Activities.This report covers a 3-month period of inspection by resident inspectors and announcedbaseline inspections by a regional radiation specialist inspector. Five Green findings, all of
Inspectors:         R. Michael Morris, Senior Resident Inspector
which were associated with non-cited violations (NCVs) were identified. The significance of
                    T. Steadham, Resident Inspector
                    A. Wilson, NRC Headquarters
                    M. Franke, Senior Resident Inspector, Perry
                    M. Jordan, NRC Consultant
                    R. Langstaff, Senior Reactor Inspector
                    M. Mitchell, Radiation Specialist
Approved by:         C. Lipa, Chief
                    Branch 4
                    Division of Reactor Projects
                                                                  Enclosure
 
                                      SUMMARY OF FINDINGS
IR 05000341/2006003; 04/01/2006-06/30/2006; Fermi Power Plant, Unit 2; Fire Protection,
Maintenance Risk Assessment, Operability Evaluations, Refueling and Outage Activities.
This report covers a 3-month period of inspection by resident inspectors and announced
baseline inspections by a regional radiation specialist inspector. Five Green findings, all of
which were associated with non-cited violations (NCVs) were identified. The significance of
most findings is indicated by their color (Green, White, Yellow, Red) using Inspection
most findings is indicated by their color (Green, White, Yellow, Red) using Inspection
Manual Chapter 0609, "Significance Determination Process" (SDP).  Findings for which the
Manual Chapter 0609, Significance Determination Process (SDP). Findings for which the
SDP does not apply may be Green after
SDP does not apply may be Green after NRC management review. The NRCs program for
NRC management review.  The NRC's program foroverseeing the safe operation of commercial nuclear power reactors is described in
overseeing the safe operation of commercial nuclear power reactors is described in
NUREG-1649, "Reactor Oversight Process," Revision 3, dated July 2000.A.NRC-Identified and Self-Revealed FindingsCornerstone:  Initiating Events*Green.  The inspectors identified an NCV of 10 CFR 50.65(a)(4) for the failure toperform an adequate risk assessment for the Division I battery load test.  The licensee
NUREG-1649, Reactor Oversight Process, Revision 3, dated July 2000.
failed to consider the effect the test would have on the temperature in the reactor
A.      NRC-Identified and Self-Revealed Findings
protection system motor generator set rooms.  Consequently, the load bank used for thetest caused the room temperature to increase which necessitated the unanticipatedinstallation of a temporary fan to cool the room.  The licensee entered this issue into
        Cornerstone: Initiating Events
their corrective action program to evaluate any programmatic or procedural deficiencies
*      Green. The inspectors identified an NCV of 10 CFR 50.65(a)(4) for the failure to
that may have contributed to this event.This finding is more than minor because the licensee's risk assessment failed toconsider maintenance activities that could increase the likelihood of an initiating event,
        perform an adequate risk assessment for the Division I battery load test. The licensee
specifically a loss of shutdown cooling from a reactor protection system motor generatorset trip on high temperature.  The finding is of very low safety significance because it did
        failed to consider the effect the test would have on the temperature in the reactor
not affect the ability
        protection system motor generator set rooms. Consequently, the load bank used for the
        test caused the room temperature to increase which necessitated the unanticipated
        installation of a temporary fan to cool the room. The licensee entered this issue into
        their corrective action program to evaluate any programmatic or procedural deficiencies
        that may have contributed to this event.
        This finding is more than minor because the licensees risk assessment failed to
        consider maintenance activities that could increase the likelihood of an initiating event,
        specifically a loss of shutdown cooling from a reactor protection system motor generator
        set trip on high temperature. The finding is of very low safety significance because it did
        not affect the ability of operators to recover from a loss of shutdown cooling if it had
        occurred. The cause of the finding is related to the cross-cutting element of Human
        Performance. (Section 1R13.2)
        Cornerstone: Mitigating Systems
*      Green. The inspectors identified an NCV of license condition 2.C(9) due to the
        presence of unauthorized transient combustible materials in the residual heat removal
        complex. An office chair and a plastic trash bin half filled with paper were secured next
        to the electrical panel and associated cable raceway for emergency diesel generator 12
        ventilation in the emergency diesel generator 12 switchgear room. The licensee entered
        this issue into their corrective action program and removed the unauthorized transient
        combustible materials from the residual heat removal complex.
        This finding is more than minor because it affected the Mitigating Systems Cornerstone
        attribute for protection against external factors. Specifically, a fire involving the
        unauthorized transient combustibles could have affected a nearby electrical panel and
        associated cable raceway containing mitigating system equipment important to safety.
                                                  2                                        Enclosure
 
  The finding is of very low safety significance because the unauthorized transient
  combustible materials would not have ignited from existing sources of heat or electrical
  energy. The cause of the finding is related to the cross-cutting element of Problem
  Identification and Resolution. (Section 1R05.2)
* Green. The inspectors identified an NCV of Technical Specification 3.1.5.a.2,
  Amendment 38, for the standby liquid control (SLC) system being inoperable for longer
  than the allowed time without the plant being placed in hot shutdown. The licensee
  failed to properly evaluate the operability of SLC during sparging activities when the
  issue was raised
using the Fermi Standardized Plant Analysis Risk (SPAR) Model, Level 1, Revision 3P,
using the Fermi Standardized Plant Analysis Risk (SPAR) Model, Level 1, Revision 3P,
Change 3.21, created October 2005. The SRA ran the SPAR model assuming common
Change 3.21, created October 2005. The SRA ran the SPAR model assuming common
cause failure of both SLC pumps, with an exposure time of 90 hours. Using the above
cause failure of both SLC pumps, with an exposure time of 90 hours. Using the above
information the SRA obtained a change in core damage frequency (CDF) of 3.1E-8(Green) for internal events. The dominant sequences involved a failure of the reactor to
information the SRA obtained a change in core damage frequency (CDF) of 3.1E-8
(Green) for internal events. The dominant sequences involved a failure of the reactor to
scram after a transient, loss of condenser heat sink, and loss of main feedwater, and
scram after a transient, loss of condenser heat sink, and loss of main feedwater, and
failure of the SLC system.   Anticipated transient without scram events are not assumed to be caused by externalevents and, therefore, the risk contribution from external events is insignificant. Similarly, because the internal events CDF is less than 1E-7, large early releasefrequency (LERF) is not significant per IMC 0609, Appendix H. The SRA concludedthe total CDF considering internal events, external events, and LERF is estimated at3.1E-8 (Green).Enforcement: Technical Specification 3.1.5.a.2, Amendment 38, required that while inModes 1 and 2, with the SLC system otherwise inoperable, the licensee must restore
failure of the SLC system.
the system to operable status within 8 hours or be in at least hot shutdown within thenext 12 hours and was in effect on August 24 and 25, 1999. Contrary to the above,
Anticipated transient without scram events are not assumed to be caused by external
beginning on August 24, 1999, and continuing until August 25, 1999, while in Modes 1  
events and, therefore, the risk contribution from external events is insignificant.
Enclosure 19and 2, the SLC system was inoperable for 21 hours while the SLC tank was being airsparged; therefore, on August 25, 1999, with the SLC system inoperable for greaterthan 20 hours, the plant was not in at least hot shutdown. Because this violation is ofvery low safety significance and because it was entered into the licensee's corrective
Similarly, because the internal events CDF is less than 1E-7, large early release
action program as CARD 06-23785, this finding is being treated as an NCV, consistent
frequency (LERF) is not significant per IMC 0609, Appendix H. The SRA concluded
with Section VI.A.1 of the NRC Enforcement Policy: NCV 05000341/2006003-04: Improper Evaluation of Standby Liquid Control Operability During Tank Sparging. .3Inappropriate Use of Risk in Operability Evaluations  a. Inspection ScopeThe inspectors reviewed CARD 06-23913 to ensure that the identified condition did notrender the involved equipment inoperable or result in an unrecognized increase in plant
the total CDF considering internal events, external events, and LERF is estimated at
risk and that the licensee appropriately applied TS limitations and appropriately returned
3.1E-8 (Green).
the affected equipment to an operable status.These activities represented one operability evaluation inspection sample.Introduction: The inspectors identified an Unresolved Item (URI) when the licenseeremoved pipe insulation, credited for environmental qualification of nearby equipment,
Enforcement: Technical Specification 3.1.5.a.2, Amendment 38, required that while in
while at power without an adequate engineering evaluation.Description: On June 8, 2006, the licensee initiated CARD 06-23913 to request a workrequest to replace contaminated insulation on the suction and discharge pipe for the "B"
Modes 1 and 2, with the SLC system otherwise inoperable, the licensee must restore
RHR pump. As a result, Work Request (WR) 000Z062027 was released and workbegan on June 13, 2006. While performing a plant tour on June 15, 2006, the
the system to operable status within 8 hours or be in at least hot shutdown within the
inspectors identified the insulation was missing from the suction pipe for the "B" RHR
next 12 hours and was in effect on August 24 and 25, 1999. Contrary to the above,
pump and questioned the licensee if the insulation removal had an approved
beginning on August 24, 1999, and continuing until August 25, 1999, while in Modes 1
engineering evaluation. Because the equipment was in a potentially harsh environment,the uninsulated pipe would increase the temperature profile of the room during accident
                                          18                                        Enclosure
conditions which could affect the environmental qualification of electrical equipment in
 
the room. The licensee stated the evaluation was documented in CARD 06-23913 and
    and 2, the SLC system was inoperable for 21 hours while the SLC tank was being air
concluded that removing the insulation while at power was acceptable.The inspectors reviewed the subject evaluation and became concerned that one of theassumptions for the evaluation was that an accident was not considered as credible
    sparged; therefore, on August 25, 1999, with the SLC system inoperable for greater
during the period of time the insulation was to be removed. Upon further review, the
    than 20 hours, the plant was not in at least hot shutdown. Because this violation is of
inspectors learned the licensee used non-accident heat loads to determine the
    very low safety significance and because it was entered into the licensees corrective
environmental effects of removing the insulation. The licensee's justification was that if
    action program as CARD 06-23785, this finding is being treated as an NCV, consistent
the total time the insulation was removed was less than 168 hours, then the probabilityof either a high energy line break or loss of coolant accident was negligible and, hence,
    with Section VI.A.1 of the NRC Enforcement Policy: NCV 05000341/2006003-04:
did not need to be assumed to occur.The definition of operability stated, however, the equipment must be capable ofperforming its specified function(s). The inherent assumption was the occurrence,
    Improper Evaluation of Standby Liquid Control Operability During Tank Sparging.
conditions, or event would exist and the safety function could be performed. Therefore,
.3  Inappropriate Use of Risk in Operability Evaluations
Enclosure 20the inspectors concluded the use of probabilities of the occurrence of accidents whilethe insulation was removed was an unacceptable assumption in the subsequent
  a. Inspection Scope
operability evaluation.While reviewing this evaluation, the inspectors discovered the licensee used thesame method of evaluating on-line insulation removal since at least September 20,
    The inspectors reviewed CARD 06-23913 to ensure that the identified condition did not
2001, and found five additional CARDs where the licensee approved removing
    render the involved equipment inoperable or result in an unrecognized increase in plant
insulation from equipment in potentially harsh areas while at power, likewise with
    risk and that the licensee appropriately applied TS limitations and appropriately returned
unacceptable evaluations. Because the extent of condition of this issue is potentiallysignificant and could extend to work other than on-line insulation removal, this item is
    the affected equipment to an operable status.
unresolved pending the inspectors' review of the licensee's full extent of condition
    These activities represented one operability evaluation inspection sample.
review and subsequent risk evaluation and is identified as Unresolved Item
    Introduction: The inspectors identified an Unresolved Item (URI) when the licensee
(URI) 05000341/2006003-05: Inappropriate Use of Risk in Operability Evaluations.1R19Post-Maintenance Testing (71111.19)  a.Inspection ScopeThe inspectors reviewed post-maintenance testing (PMT) activities associated with thefollowing scheduled maintenance:*Division I Switchyard Modifications, EDP 31880;*Feedwater Check Valve PMT, WR T210040100;
    removed pipe insulation, credited for environmental qualification of nearby equipment,
*Drywell Cooler Number 4 Replacement, WR 000Z052131;
    while at power without an adequate engineering evaluation.
*Reactor Core Isolation Cooling PMT;
    Description: On June 8, 2006, the licensee initiated CARD 06-23913 to request a work
*Reactor Recirculation Pump Discharge Valve B310SF031A, Stem Replacement,WR 000Z050487;*Main Steam Isolation Valve (MSIV), Limit Switch Replacement; and  
    request to replace contaminated insulation on the suction and discharge pipe for the B
*WR 000Z060156, Replace Control Rod Drive Pump Inboard Bearing Oil LevelSight glass.The inspectors reviewed the scope of the work performed and evaluated the adequacyof the specified PMT. The inspectors verified the PMT was performed in accordance
    RHR pump. As a result, Work Request (WR) 000Z062027 was released and work
with approved procedures, the procedures clearly stated acceptance criteria, and the
    began on June 13, 2006. While performing a plant tour on June 15, 2006, the
acceptance criteria were met. The inspectors interviewed operations, maintenance, and
    inspectors identified the insulation was missing from the suction pipe for the B RHR
engineering department personnel and reviewed the completed PMT documentation.In addition, the inspectors verified PMT problems were entered into the corrective actionprogram with the appropriate significance characterization.These activities represented seven PMT inspection samples.  b.  Findings
    pump and questioned the licensee if the insulation removal had an approved
No findings of significance were identified.  
    engineering evaluation. Because the equipment was in a potentially harsh environment,
Enclosure 211R20Refueling and Outage Activities (71111.20)  .1Routine Refueling Outage Inspection Activities  a.Inspection ScopeThe inspectors observed the licensee's performance during RF11, which was inprogress at the beginning of this inspection and concluded on May 5, 2006.This inspection consisted of a review of the licensee's outage schedule, safe shutdownplan and administrative procedures governing the outage, periodic observations of
    the uninsulated pipe would increase the temperature profile of the room during accident
equipment alignment, and plant and control room outage activities. Specifically, the
    conditions which could affect the environmental qualification of electrical equipment in
inspectors determined whether the licensee effectively managed elements of shutdown
    the room. The licensee stated the evaluation was documented in CARD 06-23913 and
risk pertaining to reactivity control, decay heat removal, inventory control, electrical
    concluded that removing the insulation while at power was acceptable.
power control, and containment integrity. The inspectors performed the following activities daily, during the outage:
    The inspectors reviewed the subject evaluation and became concerned that one of the
*attended control room operator and outage management turnover meetings toverify the current shutdown risk status was well understood and communicated;*performed walkdowns of the main control room to observe the alignment of systems important to shutdown risk;*observed the operability of reactor coolant system (RCS) instrumentation andcompared channels and trains against one another;*performed walkdowns of the turbine, auxiliary, and reactor buildings and thedrywell to observe ongoing work activities, to ensure work activities were
    assumptions for the evaluation was that an accident was not considered as credible
performed in accordance with plant procedures, and to verify procedural
    during the period of time the insulation was to be removed. Upon further review, the
requirements regarding fire protection, foreign material exclusion, and the
    inspectors learned the licensee used non-accident heat loads to determine the
storage of equipment near safety-related structures, systems, and componentswere maintained;*verified the licensee maintained secondary containment in accordance with TSrequirements; and*reviewed selected issues the licensee entered into its corrective action programto verify identified problems were being entered into the program with the
    environmental effects of removing the insulation. The licensees justification was that if
appropriate characterization and significance.Additionally, the inspectors performed the following specific activities:
    the total time the insulation was removed was less than 168 hours, then the probability
*monitored refueling activities to verify the licensee adhered to establishedprocedures and TS requirements for handling of irradiated fuel;*performed drywell closeout;
    of either a high energy line break or loss of coolant accident was negligible and, hence,
*verified shutdown cooling tagouts;
    did not need to be assumed to occur.
*verified completion of restart restraint items; and
    The definition of operability stated, however, the equipment must be capable of
*observed control rod withdrawal to criticality and portions of the plant powerascension. In particular, the inspectors reviewed the licensee's restart restraint process and verifiedthe closure of selected issues. Documents reviewed during these inspection activities
    performing its specified function(s). The inherent assumption was the occurrence,
are listed at the end of this report.  
    conditions, or event would exist and the safety function could be performed. Therefore,
Enclosure 22Because inspection activities for this refueling outage constituted one inspection samplein Inspection Report 05000341/2006002, and since only one sample is counted per
                                            19                                    Enclosure
outage, the inspection activities for this inspection period do not constitute an additional
 
refueling and outage inspection sample. b. FindingsIntroduction: The inspectors identified a Green NCV of Technical Specification 5.4.1.a,for the failure to adequately control the modification of the ventilation equipment used tovent airborne radioactive particulate to the refuel floor during reactor vessel floodup.Description: At 1450, on March 26, 2006, operators initiated core spray at approximately3000 gpm to raise reactor water level, to permit removal of the reactor vessel head. The
    the inspectors concluded the use of probabilities of the occurrence of accidents while
reactor vessel head vent pipe had been disconnected, to permit installation of a
    the insulation was removed was an unacceptable assumption in the subsequent
ventilation unit for the venting of gases to the refuel floor. The ventilation unit consisted
    operability evaluation.
of a nominal 3600 scfm fan, a charcoal filter, and a HEPA particulate filter. Neither filter
    While reviewing this evaluation, the inspectors discovered the licensee used the
had been recently tested. The ventilation unit was configured with two hoses placed to
    same method of evaluating on-line insulation removal since at least September 20,
take suction close to the reactor vessel head vent. The exhaust of the ventilation unit
    2001, and found five additional CARDs where the licensee approved removing
ran to a point below an intake for the Standby Gas Treatment System (SGTS), to permit
    insulation from equipment in potentially harsh areas while at power, likewise with
capture of the exhaust by the SGTS. At approximately 1500, the ventilation unit intake hoses were observed being pushedaway from the reactor vessel head vent, due to flow from the vent. Core spray was shut
    unacceptable evaluations. Because the extent of condition of this issue is potentially
down at 1502 and at 1504 visible moisture was seen being emitted from the vent. A
    significant and could extend to work other than on-line insulation removal, this item is
continuous air monitor on the refuel floor alarmed at 1510 and RP ordered the
    unresolved pending the inspectors review of the licensees full extent of condition
evacuation of all but essential personnel from the refuel floor. By 1525 all personnel
    review and subsequent risk evaluation and is identified as Unresolved Item
were removed from the floor and shortly after this, the entire reactor building was
    (URI) 05000341/2006003-05: Inappropriate Use of Risk in Operability Evaluations.
evacuated due to the spread of contamination. Decontamination of several workers wasrequired. Twenty-eight workers were whole body counted, with 26 showing uptakes ofvarying levels of Co-60, Co-58, and Mn-54.There were three conditions that contributed to the cause of the event. First of all,coolant activity levels were higher than expected due to a "crud burst" during shutdown
1R19 Post-Maintenance Testing (71111.19)
and the temporary loss of RWCS allowed Co-60 to enter and remain in the coolant,
  a. Inspection Scope
possibly plating out on reactor internals. The second condition related to the
    The inspectors reviewed post-maintenance testing (PMT) activities associated with the
temperature of the material vented from the reactor vessel head. Reactor vessel
    following scheduled maintenance:
outside shell temperatures indicated 215 degrees F, which equates to internal metal
    *       Division I Switchyard Modifications, EDP 31880;
temperatures above the atmospheric boiling point of water. This indicates that some ofthe coolant flashed to steam as the level in the reactor vessel rose, which could increase
    *       Feedwater Check Valve PMT, WR T210040100;
the carryover of coolant activity to the vented gas. The third condition was the
    *       Drywell Cooler Number 4 Replacement, WR 000Z052131;
inadequate processing of vented material from the reactor vessel head. The venting of
    *       Reactor Core Isolation Cooling PMT;
the airborne radioactive particulate would not have resulted in building contamination
    *       Reactor Recirculation Pump Discharge Valve B310SF031A, Stem Replacement,
and personnel uptakes if the ventilation unit had effectively removed this material to the
            WR 000Z050487;
SGTS. The use of the ventilation system was not in accordance with its design configuration. The ventilation system for previ
    *       Main Steam Isolation Valve (MSIV), Limit Switch Replacement; and
ous outages had suction hoses  
    *       WR 000Z060156, Replace Control Rod Drive Pump Inboard Bearing Oil Level
connected to
            Sight glass.
a hood thatwas placed over the reactor vessel head vent, to improve the capture of vented material.  
    The inspectors reviewed the scope of the work performed and evaluated the adequacy
The use of the hood was discontinued due to its impact on water level instrumentation.
    of the specified PMT. The inspectors verified the PMT was performed in accordance
Enclosure 23An engineering evaluation was not performed on the impact of the change inconfiguration of the ventilation system. In addition, the exhaust arrangement from theventilation unit to the SGTS had not been evaluated for effectiveness. Licensee
    with approved procedures, the procedures clearly stated acceptance criteria, and the
Procedure MES12, "Performing Temporary Modifications," requires the modification
    acceptance criteria were met. The inspectors interviewed operations, maintenance, and
process be followed and an evaluation be performed.Furthermore, licensee procedural guidance did not exist for the overall process of takingthe operating reactor to a condition allowing fuel movement. The event could have been
    engineering department personnel and reviewed the completed PMT documentation.
    In addition, the inspectors verified PMT problems were entered into the corrective action
    program with the appropriate significance characterization.
    These activities represented seven PMT inspection samples.
  b.  Findings
    No findings of significance were identified.
                                              20                                    Enclosure
 
1R20 Refueling and Outage Activities (71111.20)
  .1  Routine Refueling Outage Inspection Activities
  a. Inspection Scope
    The inspectors observed the licensees performance during RF11, which was in
    progress at the beginning of this inspection and concluded on May 5, 2006.
    This inspection consisted of a review of the licensees outage schedule, safe shutdown
    plan and administrative procedures governing the outage, periodic observations of
    equipment alignment, and plant and control room outage activities. Specifically, the
    inspectors determined whether the licensee effectively managed elements of shutdown
    risk pertaining to reactivity control, decay heat removal, inventory control, electrical
    power control, and containment integrity.
    The inspectors performed the following activities daily, during the outage:
    *       attended control room operator and outage management turnover meetings to
              verify the current shutdown risk status was well understood and communicated;
    *       performed walkdowns of the main control room to observe the alignment of
              systems important to shutdown risk;
    *       observed the operability of reactor coolant system (RCS) instrumentation and
              compared channels and trains against one another;
    *       performed walkdowns of the turbine, auxiliary, and reactor buildings and the
              drywell to observe ongoing work activities, to ensure work activities were
              performed in accordance with plant procedures, and to verify procedural
              requirements regarding fire protection, foreign material exclusion, and the
              storage of equipment near safety-related structures, systems, and components
              were maintained;
    *       verified the licensee maintained secondary containment in accordance with TS
              requirements; and
    *       reviewed selected issues the licensee entered into its corrective action program
              to verify identified problems were being entered into the program with the
              appropriate characterization and significance.
    Additionally, the inspectors performed the following specific activities:
    *       monitored refueling activities to verify the licensee adhered to established
              procedures and TS requirements for handling of irradiated fuel;
    *       performed drywell closeout;
    *       verified shutdown cooling tagouts;
    *       verified completion of restart restraint items; and
    *       observed control rod withdrawal to criticality and portions of the plant power
              ascension.
    In particular, the inspectors reviewed the licensees restart restraint process and verified
    the closure of selected issues. Documents reviewed during these inspection activities
    are listed at the end of this report.
                                                21                                      Enclosure
 
  Because inspection activities for this refueling outage constituted one inspection sample
  in Inspection Report 05000341/2006002, and since only one sample is counted per
  outage, the inspection activities for this inspection period do not constitute an additional
  refueling and outage inspection sample.
b. Findings
  Introduction: The inspectors identified a Green NCV of Technical Specification 5.4.1.a,
  for the failure to adequately control the modification of the ventilation equipment used to
  vent airborne radioactive particulate to the refuel floor during reactor vessel floodup.
  Description: At 1450, on March 26, 2006, operators initiated core spray at approximately
  3000 gpm to raise reactor water level, to permit removal of the reactor vessel head. The
  reactor vessel head vent pipe had been disconnected, to permit installation of a
  ventilation unit for the venting of gases to the refuel floor. The ventilation unit consisted
  of a nominal 3600 scfm fan, a charcoal filter, and a HEPA particulate filter. Neither filter
  had been recently tested. The ventilation unit was configured with two hoses placed to
  take suction close to the reactor vessel head vent. The exhaust of the ventilation unit
  ran to a point below an intake for the Standby Gas Treatment System (SGTS), to permit
  capture of the exhaust by the SGTS.
  At approximately 1500, the ventilation unit intake hoses were observed being pushed
  away from the reactor vessel head vent, due to flow from the vent. Core spray was shut
  down at 1502 and at 1504 visible moisture was seen being emitted from the vent. A
  continuous air monitor on the refuel floor alarmed at 1510 and RP ordered the
  evacuation of all but essential personnel from the refuel floor. By 1525 all personnel
  were removed from the floor and shortly after this, the entire reactor building was
  evacuated due to the spread of contamination. Decontamination of several workers was
  required. Twenty-eight workers were whole body counted, with 26 showing uptakes of
  varying levels of Co-60, Co-58, and Mn-54.
  There were three conditions that contributed to the cause of the event. First of all,
  coolant activity levels were higher than expected due to a crud burst during shutdown
  and the temporary loss of RWCS allowed Co-60 to enter and remain in the coolant,
  possibly plating out on reactor internals. The second condition related to the
  temperature of the material vented from the reactor vessel head. Reactor vessel
  outside shell temperatures indicated 215 degrees F, which equates to internal metal
  temperatures above the atmospheric boiling point of water. This indicates that some of
  the coolant flashed to steam as the level in the reactor vessel rose, which could increase
  the carryover of coolant activity to the vented gas. The third condition was the
  inadequate processing of vented material from the reactor vessel head. The venting of
  the airborne radioactive particulate would not have resulted in building contamination
  and personnel uptakes if the ventilation unit had effectively removed this material to the
  SGTS.
  The use of the ventilation system was not in accordance with its design configuration.
  The ventilation system for previous outages had suction hoses connected to a hood that
  was placed over the reactor vessel head vent, to improve the capture of vented material.
  The use of the hood was discontinued due to its impact on water level instrumentation.
                                            22                                      Enclosure
 
An engineering evaluation was not performed on the impact of the change in
configuration of the ventilation system. In addition, the exhaust arrangement from the
ventilation unit to the SGTS had not been evaluated for effectiveness. Licensee
Procedure MES12, Performing Temporary Modifications, requires the modification
process be followed and an evaluation be performed.
Furthermore, licensee procedural guidance did not exist for the overall process of taking
the operating reactor to a condition allowing fuel movement. The event could have been
prevented if appropriate acceptance criteria for allowable reactor vessel temperature
prevented if appropriate acceptance criteria for allowable reactor vessel temperature
and coolant activity levels existed. Thus, the root cause of the event was determined tobe a procedural and programmatic weakness.The licensee initiated CARD 06-21534, "Continuous Air Monitor Alarm on RefuelingFloor," to track the investigation of the event in their CAP. The primary corrective action
and coolant activity levels existed. Thus, the root cause of the event was determined to
be a procedural and programmatic weakness.
The licensee initiated CARD 06-21534, Continuous Air Monitor Alarm on Refueling
Floor, to track the investigation of the event in their CAP. The primary corrective action
recommendation is to develop and implement an acceptable methodology for raising
recommendation is to develop and implement an acceptable methodology for raising
reactor vessel water level. In addition, the design and configuration of the current
reactor vessel water level. In addition, the design and configuration of the current
ventilation exhaust capture system will be evaluated and modified, as appropriate toassure that it is adequate for the expected reactor vessel fill rate and radioactivematerial concentrations. The methodology may involve an alternate vent path, such as
ventilation exhaust capture system will be evaluated and modified, as appropriate to
using the attached piping to vent the reactor vessel to the drywell. Analysis: The inspectors determined the licensee's lack of control of the TemporaryModification process constituted a design control issue. The licensee's failure to
assure that it is adequate for the expected reactor vessel fill rate and radioactive
material concentrations. The methodology may involve an alternate vent path, such as
using the attached piping to vent the reactor vessel to the drywell.
Analysis: The inspectors determined the licensees lack of control of the Temporary
Modification process constituted a design control issue. The licensees failure to
adequately control the process used to vent airborne radioactive particulate to the refuel
adequately control the process used to vent airborne radioactive particulate to the refuel
floor during reactor vessel floodup represents a performance deficiency as defined in
floor during reactor vessel floodup represents a performance deficiency as defined in
NRC Inspection Manual Chapter 0612, Appendix B, "Issue Screening.The issue wasdetermined to be more than minor because if left uncorrected the issue could become a
NRC Inspection Manual Chapter 0612, Appendix B, Issue Screening. The issue was
determined to be more than minor because if left uncorrected the issue could become a
more significant safety concern if coolant activity levels were higher or if the vessel was
more significant safety concern if coolant activity levels were higher or if the vessel was
flooded quicker. The finding was assessed using NRC Inspection Manual Chapter 0609, Appendix C,"Occupational Radiation Safety Significance Determination Process" due to individual
flooded quicker.
worker unplanned, unintended dose. The finding was determined to be of very low
The finding was assessed using NRC Inspection Manual Chapter 0609, Appendix C,
safety significance because the inspectors answered, "NO," to all four phase 1
Occupational Radiation Safety Significance Determination Process due to individual
screening questions.Enforcement: Technical Specification 5.4.1.a requires that procedures recommended inRegulatory Guide 1.33, Revision 2, Appendix A, February 1978, be established,implemented and maintained.   Section 4.a of that document, in part requires
worker unplanned, unintended dose. The finding was determined to be of very low
instructions for filling, venting, and draining the reactor pressure vessel. Contrary to theabove, the initial installation of the ventilation system and the changes made to theventilation system that was used as part of the reactor vessel floodup during outageswas not processed through the Temporary Modification Procedure. This finding is being
safety significance because the inspectors answered, NO, to all four phase 1
treated as an NCV, consistent with Section VI.A.1 of the NRC Enforcement Policy and isidentified as NCV 05000341/2006003-06: Inadequate Controls for Venting the ReactorPressure Vessel Head. This issue is in the licensee's corrective action program as
screening questions.
CARD 06-22667.  
Enforcement: Technical Specification 5.4.1.a requires that procedures recommended in
Enclosure 24 .2Forced Outage 06-01  a.Inspection ScopeThe inspectors observed the licensee's performance during Forced Outage 06-01 fromMay 20, 2006, through May 29, 2006, which was scheduled to locate and replace a
Regulatory Guide 1.33, Revision 2, Appendix A, February 1978, be established,
failed fuel assembly. During power ascension following RF11, operators identified a
implemented and maintained. Section 4.a of that document, in part requires
potential fuel leak because off gas radiation levels were slightly elevated from normal.  
instructions for filling, venting, and draining the reactor pressure vessel. Contrary to the
Operators began suppression testing later that day, which identified the failed assembly.  
above, the initial installation of the ventilation system and the changes made to the
Operators initiated a manual unit shutdown to replace the failed fuel. While the unit was
ventilation system that was used as part of the reactor vessel floodup during outages
shutdown, additional assemblies subjected to similar flux profile histories were also
was not processed through the Temporary Modification Procedure. This finding is being
replaced although fuel sipping operations identified only one fuel assembly with a fuel
treated as an NCV, consistent with Section VI.A.1 of the NRC Enforcement Policy and is
cladding defect.This inspection consisted of a review of the licensee's outage schedule, safe shutdownplan and administrative procedures governing the outage, periodic observations of
identified as NCV 05000341/2006003-06: Inadequate Controls for Venting the Reactor
equipment alignment, and plant and control room outage activities. Specifically, the
Pressure Vessel Head. This issue is in the licensees corrective action program as
inspectors determined whether the licensee effectively managed elements of shutdown
CARD 06-22667.
risk pertaining to reactivity control, decay heat removal, inventory control, electrical
                                          23                                    Enclosure
power control, and containment integrity. The inspectors performed the same daily activities, during the outage as described inSection 1R20.1 for the refueling outage.These activities represented one forced outage inspection sample.  b.FindingsNo findings of significance were identified. .3Forced Outage 06-02
 
    a.Inspection ScopeThe inspectors observed the licensee's performance during Forced Outage 06-02 from
.2  Forced Outage 06-01
June 15, 2006, through June 17, 2006. On June 15, a reactor scram occurred due to a
  a. Inspection Scope
main turbine generator trip which occurred when main unit transformer 2B failed. The
    The inspectors observed the licensees performance during Forced Outage 06-01 from
inspectors responded to the control room and to the transformer area to assess the
    May 20, 2006, through May 29, 2006, which was scheduled to locate and replace a
licensee's response to the event.This inspection consisted of a review of the licensee's outage schedule, safe shutdownplan and administrative procedures governing the outage, and plant and control roomoutage activities. Specifically, the inspectors determined whether the licensee
    failed fuel assembly. During power ascension following RF11, operators identified a
effectively managed elements of shutdown risk pertaining to reactivity control, decay
    potential fuel leak because off gas radiation levels were slightly elevated from normal.
heat removal, inventory control, and electrical power control.
    Operators began suppression testing later that day, which identified the failed assembly.
Enclosure 25The inspectors performed the following activities during the outage:*attended control room operator and outage management turnover meetings toverify the current shutdown risk status was well understood and communicated;*performed walkdowns of the main control room to observe the alignment of systems important to shutdown risk;*observed the operability of RCS instrumentation and compared channels andtrains against one another; and *observed control rod withdrawal to criticality and portions of the plant powerascension.These activities represented one forced outage inspection sample.  b.FindingsNo findings of significance were identified.1R22Surveillance Testing (71111.22Q)  a.Inspection ScopeThe inspectors reviewed the test results for the following activities to determine whetherrisk-significant systems and equipment were capable of performing their intended safetyfunction and to verify testing was conducted in accordance with applicable procedural
    Operators initiated a manual unit shutdown to replace the failed fuel. While the unit was
and TS requirements:*MSIV Limit Switch (routine);*SLC Squib Valve Test (routine);
    shutdown, additional assemblies subjected to similar flux profile histories were also
*Integrity Test for Containment Penetrations X-7A, X-7B, X-7C, and X-7D (LLRT);
    replaced although fuel sipping operations identified only one fuel assembly with a fuel
*Scram Nitrogen Accumulator Integrity Test (routine);
    cladding defect.
*Scram Discharge Volume Vent and Drain Valves Operability (routine);*Secondary Containment Integrity Test (LLRT);
    This inspection consisted of a review of the licensees outage schedule, safe shutdown
*MSIV Channel Functional Test (isolation valve);
    plan and administrative procedures governing the outage, periodic observations of
*LOOP/LOCA Test (routine);
    equipment alignment, and plant and control room outage activities. Specifically, the
*Reactor Core Isolation Cooling System Automatic Actuation and Flow Test(routine); and *High Pressure Coolant Injection Flow Rate Test at 165 psig Reactor SteamPressure (routine).The inspectors reviewed the test methodology and test results to verify equipmentperformance was consistent with safety analysis and design basis assumptions. In
    inspectors determined whether the licensee effectively managed elements of shutdown
addition, the inspectors verified surveillance testing problems were being entered intothe corrective action program with the appropriate significance characterization.These activities represented seven routine, two local leak rate test (LLRT), and onecontainment isolation valve surveillance inspection samples.  
    risk pertaining to reactivity control, decay heat removal, inventory control, electrical
Enclosure 26  b.FindingsNo findings of significance were identified.1EP6Drill Evaluation (71114.06) a.Inspection ScopeThe inspectors observed the licensee perform classifications and protective actionrecommendations during licensed operator requalification training on June 20, 2006.
    power control, and containment integrity.
The inspectors observed activities in the control room simulator. The inspectors also
    The inspectors performed the same daily activities, during the outage as described in
attended the post-drill critique in the simulator. The focus of the inspectors' activitieswas to note any weaknesses and deficiencies in the shift manager's performance as
    Section 1R20.1 for the refueling outage.
emergency director and ensure the licensee evaluators noted the same weaknesses
    These activities represented one forced outage inspection sample.
and deficiencies and entered them into the corrective action program. As part of the
  b. Findings
inspection, the inspectors reviewed the drill package included in the list of documentsreviewed at the end of this report.These activities represented one drill evaluation inspection sample. b.FindingsNo findings of significance were identified.2OS1Access Control to Radiologically Significant Areas (IP 71121.01).1Plant Walkdowns and Radiation Work Permit Reviews a.Inspection ScopeThe inspectors reviewed licensee controls and surveys in the following threeradiologically significant work areas within radiation areas, high radiation areas and
    No findings of significance were identified.
airborne radioactivity areas in the plant and reviewed work packages which included
.3  Forced Outage 06-02
associated licensee controls and surveys of these areas to determine if radiological
a. Inspection Scope
controls including surveys, postings and barricades were acceptable: *Turbine Building Main Steam Reheater Replacement;*Drywell Activities; and
    The inspectors observed the licensees performance during Forced Outage 06-02 from
*Refuel Floor Activities. These activities represented one inspection sample.
    June 15, 2006, through June 17, 2006. On June 15, a reactor scram occurred due to a
The inspectors reviewed the radiation work permits (RWPs) and work packages used toaccess the three areas and other high radiation work areas to identify the work control
    main turbine generator trip which occurred when main unit transformer 2B failed. The
instructions and control barriers that had been specified. Electronic dosimeter alarm set
    inspectors responded to the control room and to the transformer area to assess the
points for both integrated dose and dose rate were evaluated for conformity with survey
    licensees response to the event.
indications and plant policy. Workers were interviewed to verify they were aware of the
    This inspection consisted of a review of the licensees outage schedule, safe shutdown
actions required when their electronic dosimeters noticeably malfunctioned or alarmed.  
    plan and administrative procedures governing the outage, and plant and control room
Enclosure 27These activities represented one inspection sample.The inspectors walked down and surveyed (using an NRC survey meter) the three areasto verify the prescribed RWPs, procedure, and engineering controls were in place,
    outage activities. Specifically, the inspectors determined whether the licensee
licensee surveys and postings were complete and accurate, and air samplers were
    effectively managed elements of shutdown risk pertaining to reactivity control, decay
properly located. These activities represented one inspection sample.
    heat removal, inventory control, and electrical power control.
The inspectors reviewed RWPs for the following airborne radioactivity areas to verifybarrier integrity and engineering controls performance, e.g., high efficiency particulate
                                              24                                      Enclosure
air filter ventilati
 
on system operation, and to determine if there was a potential forindividual worker internal exposures of greater than 50 millirem committed effectivedose equivalent. There were no areas where there was a potential for individual worker
    The inspectors performed the following activities during the outage:
internal exposures of greater than 50 millirem committed effective dose equivalent. Work areas having a history of, or the potential for, airborne transuranic isotopes were
    *       attended control room operator and outage management turnover meetings to
evaluated to verify the licensee had considered the potential for transuranic isotopesand provided appropriate worker protection. There where no areas having a history of,
            verify the current shutdown risk status was well understood and communicated;
or the potential for, airborne transuranic isotopes. These activities represented one inspection sample.
    *       performed walkdowns of the main control room to observe the alignment of
The adequacy of the licensee's internal dose assessment process for any actual internalexposures greater than 50 millirem committed effective dose equivalent was assessed. There were no internal exposures greater than 50 millirem committed effective doseequivalent.  These activities represented one inspection sample. b.FindingsNo findings of significance were identified..2Problem Identification and Resolution a.Inspection ScopeThe inspectors reviewed three corrective action reports related to access controls andhigh radiation area radiological incidents. Staff members were interviewed and
            systems important to shutdown risk;
corrective action documents were reviewed to verify that follow-up activities were being
    *       observed the operability of RCS instrumentation and compared channels and
conducted in an effective and timely manner commensurate with their importance to
            trains against one another; and
safety and risk based on the following:*initial problem identification, characterization, and tracking;*disposition of operability/reportability issues;*evaluation of safety significance/risk and priority for resolution;
    *       observed control rod withdrawal to criticality and portions of the plant power
*identification of repetitive problems;  
            ascension.
*identification of contributing causes;
    These activities represented one forced outage inspection sample.
*identification and implementation of effective corrective actions;  
  b. Findings
Enclosure 28*resolution of NCVs tracked in the corrective action system; and*implementation/consideration of risk-significant operational experience feedback.These activities represented one inspection sample. b.FindingsNo findings of significance were identified. .3Job-In-Progress Reviews a.Inspection ScopeThe inspectors observed the following three jobs that were being performed in radiationareas, airborne radioactivity areas, or high radiation areas for observation of work
    No findings of significance were identified.
activities that presented the greatest radiological risk to workers: *Drywell Cooler Number Four Removal;*Cutout and Replace Check Valve E1100F031A; and
1R22 Surveillance Testing (71111.22Q)
*Perform Refuel Activities.The inspectors reviewed radiological job requirements for the three activities includingRWP requirements and work procedure requirements, and attended As-Low-As-Is-
  a. Inspection Scope
Reasonably-Achievable (ALARA) job briefings. These activities represented one inspection sample.  
    The inspectors reviewed the test results for the following activities to determine whether
Job performance was observed with respect to these requirements to verify radiologicalconditions in the work area were adequately communicated to workers through pre-job
    risk-significant systems and equipment were capable of performing their intended safety
briefings and postings. The inspectors also verified the adequacy of radiological
    function and to verify testing was conducted in accordance with applicable procedural
controls including required radiation, contamination, and airborne surveys for systembreaches; radiation protection job coverage which included audio and visual surveillancefor remote job coverage; and contamination controls. These activities represented one inspection sample. b.FindingsNo findings of significance were identified. .4Radiation Worker Performance a.Inspection ScopeDuring job performance observations, the inspectors evaluated radiation workerperformance with respect to stated radiation protection work requirements and
    and TS requirements:
evaluated whether workers were aware of the significant radiological conditions in their
    *       MSIV Limit Switch (routine);
workplace, the RWP controls and limits in place, and that their performance hadaccounted for the level of radiological hazards present.  
    *       SLC Squib Valve Test (routine);
Enclosure 29These activities represented one inspection sample.The inspectors reviewed radiological problem reports which found the cause of theevent was due to radiation worker errors to determine if there was an observable pattern
    *       Integrity Test for Containment Penetrations X-7A, X-7B, X-7C, and X-7D (LLRT);
traceable to a similar cause, and to determine if this perspective matched the corrective
    *       Scram Nitrogen Accumulator Integrity Test (routine);
action approach taken by the licensee to resolve the reported problems. These
    *       Scram Discharge Volume Vent and Drain Valves Operability (routine);
problems, along with planned and taken corrective actions were discussed with the
    *       Secondary Containment Integrity Test (LLRT);
Radiation Protection Manager. These activities represented one inspection sample. b.FindingsNo findings of significance were identified..5Radiation Protection Technician (RPT) Proficiency a.Inspection ScopeDuring job performance observations, the inspectors evaluated RPT performance withrespect to radiation protection work requirements and evaluated whether they were
    *       MSIV Channel Functional Test (isolation valve);
aware of the radiological conditions in their workplace, the RWP controls and limits in
    *       LOOP/LOCA Test (routine);
place, and if their performance was consistent with their training and qualifications withrespect to the radiological hazards and work activities. These activities represented one inspection sample.
    *       Reactor Core Isolation Cooling System Automatic Actuation and Flow Test
The inspectors reviewed two radiological problem reports which found the cause of theevent was radiation protection technician error to determine if there was an observable
            (routine); and
pattern traceable to a similar cause, and to determine if this perspective matched the
    *       High Pressure Coolant Injection Flow Rate Test at 165 psig Reactor Steam
corrective action approach taken by the licensee to resolve the reported problems. These activities represented one inspection sample. b.FindingsNo findings of significance were identified.2OS2As-Low-As-Is-Reasonably-Achievable Planning And Controls (ALARA) (IP 71121.02).1Inspection Planning a.Inspection ScopeThe inspectors reviewed plant collective exposure history, current exposure trends, ongoing and planned activities in order to assess current performance and exposure
            Pressure (routine).
challenges. This included determining the plant's current 3-year rolling average forcollective exposure in order to help establish resource allocations and to provide a
    The inspectors reviewed the test methodology and test results to verify equipment
perspective of significance for any resulting inspection finding assessment.  
    performance was consistent with safety analysis and design basis assumptions. In
Enclosure 30These activities represented one inspection sample.The inspectors reviewed the outage work scheduled during the inspection period andassociated work activity exposure estimates for the following five work activities which
    addition, the inspectors verified surveillance testing problems were being entered into
were likely to result in the highest personnel collective exposures: *Drywell Cooler Number Four Removal;*Cutout and Replace Check Valve E1100F031A;
    the corrective action program with the appropriate significance characterization.
*Refuel Floor Activities;
    These activities represented seven routine, two local leak rate test (LLRT), and one
*Main Steam Reheater Replacement; and
    containment isolation valve surveillance inspection samples.
*In-Service Inspections.These activities represented one inspection sample.
                                              25                                      Enclosure
The inspectors determined site specific trends in collective exposures and source-termmeasurements. The inspectors reviewed procedures associated with maintaining
 
occupational exposures ALARA and processes used to estimate and track work activity
  b. Findings
specific exposures. These activities represented two inspection samples. b.FindingsNo findings of significance were identified..2Radiological Work Planning a.Inspection ScopeThe inspectors evaluated the licensee's list of planned work activities for RF11 rankedby estimated exposure that were in progress and reviewed the following three work
    No findings of significance were identified.
activities of exposure significance: *06-1113, CRD Exc hange;*06-1205, East/West MSR Replacement; and
1EP6 Drill Evaluation (71114.06)
*06-1124, Drywell Cooler Number Four Removal.For these three activities, the inspectors reviewed the ALARA work activity evaluations,exposure estimates, and exposure mitigation requirements in order to verify the licensee
  a. Inspection Scope
had established procedures and engineering and work controls that were based on
    The inspectors observed the licensee perform classifications and protective action
sound radiation protection principles in order to achieve occupational exposures that
    recommendations during licensed operator requalification training on June 20, 2006.
were ALARA. This also involved determining that the licensee had reasonably grouped
    The inspectors observed activities in the control room simulator. The inspectors also
the radiological work into work activities, based on historical precedence, industry
    attended the post-drill critique in the simulator. The focus of the inspectors activities
norms, and/or special circumstances.The inspectors compared the results achieved including dose rate reductions andperson-rem used with the intended dose established in the licensee's ALARA planning
    was to note any weaknesses and deficiencies in the shift managers performance as
for these three work activities. Reasons for inconsistencies between intended and
    emergency director and ensure the licensee evaluators noted the same weaknesses
actual work activity doses were reviewed.  
    and deficiencies and entered them into the corrective action program. As part of the
Enclosure 31These activities represented one inspection sample. b.FindingsNo findings of significance were identified..3Verification of Dose Estimates and Exposure Tracking Systems a.Inspection ScopeThe licensee's process for adjusting exposure estimates or re-planning work, whenunexpected changes in scope, emergent work or higher than anticipated radiation levelswere encountered, was evaluated. This included determining that adjustments toestimated exposure (intended dose) were based on sound radiation protection and
    inspection, the inspectors reviewed the drill package included in the list of documents
ALARA principles and not adjusted to account for failures to control the work. The
    reviewed at the end of this report.
frequency of these adjustments was reviewed to evaluate the adequacy of the original
    These activities represented one drill evaluation inspection sample.
ALARA planning process. These activities represented one inspection sample. b.FindingsNo findings of significance were identified..4Job Site Inspections and ALARA Control a.Inspection ScopeThe inspectors observed the following five jobs that were being performed in radiationareas, airborne radioactivity areas, or high radiation areas for observation of work
  b. Findings
activities that presented the greatest radiological risk to workers.*Drywell Cooler Number Four Removal;*Cutout and Replace Check Valve E1100F031A;
    No findings of significance were identified.
*Refuel Floor Activities;
2OS1 Access Control to Radiologically Significant Areas (IP 71121.01)
*Main Steam Reheater Replacement; and
.1  Plant Walkdowns and Radiation Work Permit Reviews
*In-Service Inspections.The licensee's use of engineering controls to achieve dose reductions was evaluated toverify procedures and controls were consistent with the licensee's ALARA reviews,
  a. Inspection Scope
sufficient shielding of radiation sources was provided for, and the dose expended to
    The inspectors reviewed licensee controls and surveys in the following three
install/remove the shielding did not exceed the dose reduction benefits afforded by the
    radiologically significant work areas within radiation areas, high radiation areas and
shielding. These activities represented one inspection sample.   b.FindingsNo findings of significance were identified.
    airborne radioactivity areas in the plant and reviewed work packages which included
Enclosure 32.5Radiation Worker Performance   a.Inspection ScopeRadiation worker and RPT performance was observed during work activities beingperformed in radiation areas, airborne radioactivity areas, and high radiation areas that
    associated licensee controls and surveys of these areas to determine if radiological
presented the greatest radiological risk to workers. The inspectors evaluated whether
    controls including surveys, postings and barricades were acceptable:
workers demonstrated the ALARA philosophy in practice by being familiar with the workactivity scope and tools to be used, by utilizing ALARA low dose waiting areas, and thatwork activity controls were being complied with. Also, radiation worker training and skill
    *   Turbine Building Main Steam Reheater Replacement;
levels were reviewed to determine if they were sufficient relative to the radiological
    *   Drywell Activities; and
hazards and the work involved. These activities represented one inspection sample. b.FindingsNo findings of significance were identified.4.OTHER ACTIVITIES (OA)
    *   Refuel Floor Activities.
  4OA2Identification and Resolution of Problems (71152) .1Routine Review of Identification and Resolution of Problems a.  Inspection ScopeAs discussed in previous sections of this report, the inspectors routinely reviewed issuesduring baseline inspection activities and plant status reviews to verify they were being
    These activities represented one inspection sample.
entered into the licensee's corrective action system at an appropriate threshold,adequate attention was being given to timely corrective actions, and adverse trends
    The inspectors reviewed the radiation work permits (RWPs) and work packages used to
were identified and addressed.  b.  FindingsNo findings of significance were identified. .2  Semi-Annual Trend Review   a.Inspection ScopeThe inspectors performed a screening review of each item entered into the licensee'scorrective action program to identify trends that might indicate the existence of a more
    access the three areas and other high radiation work areas to identify the work control
significant safety issue. The inspectors considered repetitive or closely related issues
    instructions and control barriers that had been specified. Electronic dosimeter alarm set
that may have been documented by the licensee outside the normal corrective actionprogram, such as in:trend reports or performance indicators, major equipment problem lists,
    points for both integrated dose and dose rate were evaluated for conformity with survey
Enclosure 33repetitive and/or rework maintenance lists, departmental problem/challenges lists, system health reports, quality assurance audit/surveillance reports, self assessment reports, maintenance rule assessments, or corrective action backlog lists.The inspectors verified the licensee was identifying issues at an appropriate thresholdand entering them into their corrective action program by comparing those issues
    indications and plant policy. Workers were interviewed to verify they were aware of the
identified by the NRC during the conduct of the plant status and inspectable areaportions of the program with those issues identified by the licensee.   b.IssuesUnidentified drywell leakage was fluctuating after startup from RF11 but has sinceleveled out. From the lowest value, unidentified leakage has increased from about
    actions required when their electronic dosimeters noticeably malfunctioned or alarmed.
0.06 gpm to an average daily value of 0.14 gpm. Additionally, the inner seal pressure
                                              26                                    Enclosure
for the "B" reactor recirculation pump has been fluctuating by as much as 40-60 psig;
 
however, there does not appear to be a correlation between the seal pressure
    These activities represented one inspection sample.
oscillations and drywell leakage. These issues are in the licensee's corrective actionprogram as CARDs 06-24313 for the unidentified leakage and 06-23791 for the seal
    The inspectors walked down and surveyed (using an NRC survey meter) the three areas
pressure oscillations.4OA3Event Followup (71153).1Reactor Scram due to Main Transformer Fault a.Inspection ScopeAs described in Section 1R20.3 of this report, the inspectors responded to the controlroom on June 15, 2006, when the reactor automatically shut down as a result of the
    to verify the prescribed RWPs, procedure, and engineering controls were in place,
failure of main unit transformer 2B. The inspectors observed plant parameters and
    licensee surveys and postings were complete and accurate, and air samplers were
status, evaluated the performance of mitigating systems and licensee actions, confirmedthat the licensee properly classified the event in accordance with emergency action level
    properly located.
procedures and made timely notifications to  
    These activities represented one inspection sample.
NRC and state/county governments, asrequired by 10 CFR 50.72 (Event Number 42643). The inspectors determined and
    The inspectors reviewed RWPs for the following airborne radioactivity areas to verify
communicated details regarding the event to  
    barrier integrity and engineering controls performance, e.g., high efficiency particulate
NRC management, risk analysts andothers in Region III and Headquarters as input to an evaluation per ManagementDirective 8.3 for determining the appropriate level of event response. Based on the
    air filter ventilation system operation, and to determine if there was a potential for
events that occurred, routine resident inspection efforts were deemed appropriate. b.FindingsNo findings of significance were identified.  
    individual worker internal exposures of greater than 50 millirem committed effective
Enclosure 34.2 Review of Licensee Event Reports (LER) a.(Closed) LER 50-341/2006-001: At 0039 hours on April 1, 2006, Fermi 2 feedwater linecheck valves B2100F010A and B2100F076A failed their LLRT. The air leakage rate of
    dose equivalent. There were no areas where there was a potential for individual worker
the inboard check valve B2100F010A was 324.21 standard cubic feet per hour (SCFH),
    internal exposures of greater than 50 millirem committed effective dose equivalent.
and the leakage rate of outboard check valve B2100F076A was above the
    Work areas having a history of, or the potential for, airborne transuranic isotopes were
measurement capability of the leak rate monitor. The penetration (X-9A) minimum-pathway air leakage value was determined to be 324.21 SCFH which is greater than the
    evaluated to verify the licensee had considered the potential for transuranic isotopes
allowable containment leakage rate (La) value of 296.3 SCFH per TS 5.5.12 and higher
    and provided appropriate worker protection. There where no areas having a history of,
than the allowable secondary containment bypass leakage rate of 0.1 La or 29.63 SCFHper TS Surveillance Requirement 3.6.1.3.11. The B2100F076A failure was attributed tosoft seat degradation which was primarily caused by extending its service time to three
    or the potential for, airborne transuranic isotopes.
operating cycles. The B2100F010A valve failure was attributed to soft seat degradationdue to a slight misalignment of the valve disc to the in-body seat, compounded by wear
    These activities represented one inspection sample.
between the internal shaft and valve disc. The slight misalignment caused the soft seat
    The adequacy of the licensees internal dose assessment process for any actual internal
along the top portion of the disc to contact the seat first, resulting in a scraping action as
    exposures greater than 50 millirem committed effective dose equivalent was assessed.
the disc flexed to its full seat position. For both valves, the soft seats were replaced,
    There were no internal exposures greater than 50 millirem committed effective dose
and the soft seat service time has been limited to two operating cycles. The internalshaft for the B2100F010A valve was replaced, and the alignment between the disc andthe valve seat was adjusted. Both valves were retested and met their associated LLRT
    equivalent.
acceptance criteria prior to restart of the unit.The LER was reviewed by the inspectors. No findings of significance were identifiedand no violation of  
    These activities represented one inspection sample.
NRC requirements occurred. The licensee documented the LLRTfailure in CARD 06-21751. This LER is closed.4OA6Exit Meetings.1Exit Meeting SummaryOn July 11, 2006, the inspectors presented the inspection results to Mr. D. Cobb andother members of licensee management at the conclusion of the inspection. The
  b. Findings
inspectors asked the licensee whether any material examined during the inspection
    No findings of significance were identified.
should be considered proprietary. No proprietary information was identified..2Interim Exit MeetingsOn April 7, 2006, an interim exit meeting was conducted for the Access Control toRadiological Areas and ALARA inspection with Mr. Kevin Hlavaty, Plant Manager, and  
.2  Problem Identification and Resolution
other licensee staff.4OA7Licensee-Identified ViolationsThe following violation of very low significance was identified by the licensee and is aviolation of NRC requirements, which meet the criteria of Section VI of the NRCEnforcement Manual, NUREG-1600, for being dispositioned as an NCV.  
  a. Inspection Scope
Enclosure 35Cornerstone: Public Radiation SafetyThe licensee's procedure 67.000.103, "Surveying of Outgoing Shipments," directs thestaff to survey outgoing vehicles used to carry an exclusive use shipment of radioactive
    The inspectors reviewed three corrective action reports related to access controls and
material. The procedure relies on the proper identification of the incoming shipment as
    high radiation area radiological incidents. Staff members were interviewed and
an exclusive use shipment. This procedure is used to implement the requirements of
    corrective action documents were reviewed to verify that follow-up activities were being
49 CFR 173.443 and 49 CFR 177.843 that require the specific release survey of
    conducted in an effective and timely manner commensurate with their importance to
vehicles in exclusive use situations. Contrary to the above, and as described in
    safety and risk based on the following:
CARD 06-21389, on March 20, 2006, an exclusive use radioactive material shipment
    *   initial problem identification, characterization, and tracking;
was received by the licensee. The shipment contained one package of Limited Quantityradioactive material and four boxes of non-radioactive material and the radiation
    *   disposition of operability/reportability issues;
protection staff assigned to accept the shipment incorrectly identified the shipment as anon-exclusive use shipment. After the packages were removed from the conveyance,
    *   evaluation of safety significance/risk and priority for resolution;
the vehicle was released without the required survey. This was identified by licensee
    *   identification of repetitive problems;
supervision but not before the vehicle had departed the site. The carrier was contactedand the vehicle returned to the licensee's site before further transportation activity had
    *   identification of contributing causes;
commenced and a survey was completed. No contamination was found and no dose
    *   identification and implementation of effective corrective actions;
rates above background were identified. The finding is of very low safety significance
                                                27                                    Enclosure
because it did not result in an unmonitored release nor were any dose limits
 
approached.ATTACHMENT: SUPPLEMENTAL INFORMATION  
    *   resolution of NCVs tracked in the corrective action system; and
Attachment
    *   implementation/consideration of risk-significant operational experience feedback.
1KEY POINTS OF CONTACTLicenseeD. Gipson, Chief Nuclear OfficerD. Cobb, Assistant Vice President, Nuclear Generation
    These activities represented one inspection sample.
  b. Findings
    No findings of significance were identified.
.3  Job-In-Progress Reviews
  a. Inspection Scope
    The inspectors observed the following three jobs that were being performed in radiation
    areas, airborne radioactivity areas, or high radiation areas for observation of work
    activities that presented the greatest radiological risk to workers:
    *   Drywell Cooler Number Four Removal;
    *   Cutout and Replace Check Valve E1100F031A; and
    *   Perform Refuel Activities.
    The inspectors reviewed radiological job requirements for the three activities including
    RWP requirements and work procedure requirements, and attended As-Low-As-Is-
    Reasonably-Achievable (ALARA) job briefings.
    These activities represented one inspection sample.
    Job performance was observed with respect to these requirements to verify radiological
    conditions in the work area were adequately communicated to workers through pre-job
    briefings and postings. The inspectors also verified the adequacy of radiological
    controls including required radiation, contamination, and airborne surveys for system
    breaches; radiation protection job coverage which included audio and visual surveillance
    for remote job coverage; and contamination controls.
    These activities represented one inspection sample.
  b. Findings
    No findings of significance were identified.
.4  Radiation Worker Performance
  a. Inspection Scope
    During job performance observations, the inspectors evaluated radiation worker
    performance with respect to stated radiation protection work requirements and
    evaluated whether workers were aware of the significant radiological conditions in their
    workplace, the RWP controls and limits in place, and that their performance had
    accounted for the level of radiological hazards present.
                                              28                                      Enclosure
 
    These activities represented one inspection sample.
    The inspectors reviewed radiological problem reports which found the cause of the
    event was due to radiation worker errors to determine if there was an observable pattern
    traceable to a similar cause, and to determine if this perspective matched the corrective
    action approach taken by the licensee to resolve the reported problems. These
    problems, along with planned and taken corrective actions were discussed with the
    Radiation Protection Manager.
    These activities represented one inspection sample.
  b. Findings
    No findings of significance were identified.
.5  Radiation Protection Technician (RPT) Proficiency
  a. Inspection Scope
    During job performance observations, the inspectors evaluated RPT performance with
    respect to radiation protection work requirements and evaluated whether they were
    aware of the radiological conditions in their workplace, the RWP controls and limits in
    place, and if their performance was consistent with their training and qualifications with
    respect to the radiological hazards and work activities.
    These activities represented one inspection sample.
    The inspectors reviewed two radiological problem reports which found the cause of the
    event was radiation protection technician error to determine if there was an observable
    pattern traceable to a similar cause, and to determine if this perspective matched the
    corrective action approach taken by the licensee to resolve the reported problems.
    These activities represented one inspection sample.
  b. Findings
    No findings of significance were identified.
2OS2 As-Low-As-Is-Reasonably-Achievable Planning And Controls (ALARA) (IP 71121.02)
.1  Inspection Planning
  a. Inspection Scope
    The inspectors reviewed plant collective exposure history, current exposure trends,
    ongoing and planned activities in order to assess current performance and exposure
    challenges. This included determining the plants current 3-year rolling average for
    collective exposure in order to help establish resource allocations and to provide a
    perspective of significance for any resulting inspection finding assessment.
                                              29                                      Enclosure
 
    These activities represented one inspection sample.
    The inspectors reviewed the outage work scheduled during the inspection period and
    associated work activity exposure estimates for the following five work activities which
    were likely to result in the highest personnel collective exposures:
    *   Drywell Cooler Number Four Removal;
    *   Cutout and Replace Check Valve E1100F031A;
    *   Refuel Floor Activities;
    *   Main Steam Reheater Replacement; and
    *   In-Service Inspections.
    These activities represented one inspection sample.
    The inspectors determined site specific trends in collective exposures and source-term
    measurements. The inspectors reviewed procedures associated with maintaining
    occupational exposures ALARA and processes used to estimate and track work activity
    specific exposures.
    These activities represented two inspection samples.
  b. Findings
    No findings of significance were identified.
.2  Radiological Work Planning
  a. Inspection Scope
    The inspectors evaluated the licensees list of planned work activities for RF11 ranked
    by estimated exposure that were in progress and reviewed the following three work
    activities of exposure significance:
    *   06-1113, CRD Exchange;
    *   06-1205, East/West MSR Replacement; and
    *   06-1124, Drywell Cooler Number Four Removal.
    For these three activities, the inspectors reviewed the ALARA work activity evaluations,
    exposure estimates, and exposure mitigation requirements in order to verify the licensee
    had established procedures and engineering and work controls that were based on
    sound radiation protection principles in order to achieve occupational exposures that
    were ALARA. This also involved determining that the licensee had reasonably grouped
    the radiological work into work activities, based on historical precedence, industry
    norms, and/or special circumstances.
    The inspectors compared the results achieved including dose rate reductions and
    person-rem used with the intended dose established in the licensees ALARA planning
    for these three work activities. Reasons for inconsistencies between intended and
    actual work activity doses were reviewed.
                                              30                                    Enclosure
 
      These activities represented one inspection sample.
  b. Findings
      No findings of significance were identified.
.3    Verification of Dose Estimates and Exposure Tracking Systems
  a. Inspection Scope
      The licensees process for adjusting exposure estimates or re-planning work, when
      unexpected changes in scope, emergent work or higher than anticipated radiation levels
      were encountered, was evaluated. This included determining that adjustments to
      estimated exposure (intended dose) were based on sound radiation protection and
      ALARA principles and not adjusted to account for failures to control the work. The
      frequency of these adjustments was reviewed to evaluate the adequacy of the original
      ALARA planning process.
      These activities represented one inspection sample.
  b. Findings
      No findings of significance were identified.
.4    Job Site Inspections and ALARA Control
  a. Inspection Scope
      The inspectors observed the following five jobs that were being performed in radiation
      areas, airborne radioactivity areas, or high radiation areas for observation of work
      activities that presented the greatest radiological risk to workers.
      *   Drywell Cooler Number Four Removal;
      *   Cutout and Replace Check Valve E1100F031A;
      *   Refuel Floor Activities;
      *   Main Steam Reheater Replacement; and
      *   In-Service Inspections.
      The licensees use of engineering controls to achieve dose reductions was evaluated to
      verify procedures and controls were consistent with the licensees ALARA reviews,
      sufficient shielding of radiation sources was provided for, and the dose expended to
      install/remove the shielding did not exceed the dose reduction benefits afforded by the
      shielding.
      These activities represented one inspection sample.
  b. Findings
      No findings of significance were identified.
                                              31                                      Enclosure
 
.5    Radiation Worker Performance
  a. Inspection Scope
      Radiation worker and RPT performance was observed during work activities being
      performed in radiation areas, airborne radioactivity areas, and high radiation areas that
      presented the greatest radiological risk to workers. The inspectors evaluated whether
      workers demonstrated the ALARA philosophy in practice by being familiar with the work
      activity scope and tools to be used, by utilizing ALARA low dose waiting areas, and that
      work activity controls were being complied with. Also, radiation worker training and skill
      levels were reviewed to determine if they were sufficient relative to the radiological
      hazards and the work involved.
      These activities represented one inspection sample.
  b. Findings
      No findings of significance were identified.
4.   OTHER ACTIVITIES (OA)
  4OA2 Identification and Resolution of Problems (71152)
.1  Routine Review of Identification and Resolution of Problems
  a.  Inspection Scope
      As discussed in previous sections of this report, the inspectors routinely reviewed issues
      during baseline inspection activities and plant status reviews to verify they were being
      entered into the licensee's corrective action system at an appropriate threshold,
      adequate attention was being given to timely corrective actions, and adverse trends
      were identified and addressed.
   b.  Findings
      No findings of significance were identified.
.2  Semi-Annual Trend Review
  a. Inspection Scope
      The inspectors performed a screening review of each item entered into the licensees
      corrective action program to identify trends that might indicate the existence of a more
      significant safety issue. The inspectors considered repetitive or closely related issues
      that may have been documented by the licensee outside the normal corrective action
      program, such as in:
      C  trend reports or performance indicators,
      C  major equipment problem lists,
                                              32                                      Enclosure
 
      C    repetitive and/or rework maintenance lists,
      C    departmental problem/challenges lists,
      C    system health reports,
      C    quality assurance audit/surveillance reports,
      C    self assessment reports,
      C    maintenance rule assessments, or
      C    corrective action backlog lists.
      The inspectors verified the licensee was identifying issues at an appropriate threshold
      and entering them into their corrective action program by comparing those issues
      identified by the NRC during the conduct of the plant status and inspectable area
      portions of the program with those issues identified by the licensee.
  b. Issues
      Unidentified drywell leakage was fluctuating after startup from RF11 but has since
      leveled out. From the lowest value, unidentified leakage has increased from about
      0.06 gpm to an average daily value of 0.14 gpm. Additionally, the inner seal pressure
      for the B reactor recirculation pump has been fluctuating by as much as 40-60 psig;
      however, there does not appear to be a correlation between the seal pressure
      oscillations and drywell leakage. These issues are in the licensees corrective action
      program as CARDs 06-24313 for the unidentified leakage and 06-23791 for the seal
      pressure oscillations.
4OA3 Event Followup (71153)
.1    Reactor Scram due to Main Transformer Fault
  a. Inspection Scope
      As described in Section 1R20.3 of this report, the inspectors responded to the control
      room on June 15, 2006, when the reactor automatically shut down as a result of the
      failure of main unit transformer 2B. The inspectors observed plant parameters and
      status, evaluated the performance of mitigating systems and licensee actions, confirmed
      that the licensee properly classified the event in accordance with emergency action level
      procedures and made timely notifications to NRC and state/county governments, as
      required by 10 CFR 50.72 (Event Number 42643). The inspectors determined and
      communicated details regarding the event to NRC management, risk analysts and
      others in Region III and Headquarters as input to an evaluation per Management
      Directive 8.3 for determining the appropriate level of event response. Based on the
      events that occurred, routine resident inspection efforts were deemed appropriate.
  b. Findings
      No findings of significance were identified.
                                              33                                    Enclosure
 
.2   Review of Licensee Event Reports (LER)
  a. (Closed) LER 50-341/2006-001: At 0039 hours on April 1, 2006, Fermi 2 feedwater line
    check valves B2100F010A and B2100F076A failed their LLRT. The air leakage rate of
    the inboard check valve B2100F010A was 324.21 standard cubic feet per hour (SCFH),
    and the leakage rate of outboard check valve B2100F076A was above the
    measurement capability of the leak rate monitor. The penetration (X-9A) minimum-
    pathway air leakage value was determined to be 324.21 SCFH which is greater than the
    allowable containment leakage rate (La) value of 296.3 SCFH per TS 5.5.12 and higher
    than the allowable secondary containment bypass leakage rate of 0.1 La or 29.63 SCFH
    per TS Surveillance Requirement 3.6.1.3.11. The B2100F076A failure was attributed to
    soft seat degradation which was primarily caused by extending its service time to three
    operating cycles. The B2100F010A valve failure was attributed to soft seat degradation
    due to a slight misalignment of the valve disc to the in-body seat, compounded by wear
    between the internal shaft and valve disc. The slight misalignment caused the soft seat
    along the top portion of the disc to contact the seat first, resulting in a scraping action as
    the disc flexed to its full seat position. For both valves, the soft seats were replaced,
    and the soft seat service time has been limited to two operating cycles. The internal
    shaft for the B2100F010A valve was replaced, and the alignment between the disc and
    the valve seat was adjusted. Both valves were retested and met their associated LLRT
    acceptance criteria prior to restart of the unit.
    The LER was reviewed by the inspectors. No findings of significance were identified
    and no violation of NRC requirements occurred. The licensee documented the LLRT
    failure in CARD 06-21751. This LER is closed.
4OA6 Exit Meetings
.1  Exit Meeting Summary
    On July 11, 2006, the inspectors presented the inspection results to Mr. D. Cobb and
    other members of licensee management at the conclusion of the inspection. The
    inspectors asked the licensee whether any material examined during the inspection
    should be considered proprietary. No proprietary information was identified.
.2  Interim Exit Meetings
    On April 7, 2006, an interim exit meeting was conducted for the Access Control to
    Radiological Areas and ALARA inspection with Mr. Kevin Hlavaty, Plant Manager, and
    other licensee staff.
4OA7 Licensee-Identified Violations
    The following violation of very low significance was identified by the licensee and is a
    violation of NRC requirements, which meet the criteria of Section VI of the NRC
    Enforcement Manual, NUREG-1600, for being dispositioned as an NCV.
                                                34                                      Enclosure
 
    Cornerstone: Public Radiation Safety
    The licensees procedure 67.000.103, Surveying of Outgoing Shipments, directs the
    staff to survey outgoing vehicles used to carry an exclusive use shipment of radioactive
    material. The procedure relies on the proper identification of the incoming shipment as
    an exclusive use shipment. This procedure is used to implement the requirements of
    49 CFR 173.443 and 49 CFR 177.843 that require the specific release survey of
    vehicles in exclusive use situations. Contrary to the above, and as described in
    CARD 06-21389, on March 20, 2006, an exclusive use radioactive material shipment
    was received by the licensee. The shipment contained one package of Limited Quantity
    radioactive material and four boxes of non-radioactive material and the radiation
    protection staff assigned to accept the shipment incorrectly identified the shipment as a
    non-exclusive use shipment. After the packages were removed from the conveyance,
    the vehicle was released without the required survey. This was identified by licensee
    supervision but not before the vehicle had departed the site. The carrier was contacted
    and the vehicle returned to the licensees site before further transportation activity had
    commenced and a survey was completed. No contamination was found and no dose
    rates above background were identified. The finding is of very low safety significance
    because it did not result in an unmonitored release nor were any dose limits
    approached.
ATTACHMENT: SUPPLEMENTAL INFORMATION
                                            35                                      Enclosure
 
                                  KEY POINTS OF CONTACT
Licensee
D. Gipson, Chief Nuclear Officer
D. Cobb, Assistant Vice President, Nuclear Generation
K. Hlavaty, Plant Manager
K. Hlavaty, Plant Manager
S. Bartman, Nuclear Production
S. Bartman, Nuclear Production
Line 634: Line 1,451:
J. Korte, Manager, Nuclear Security
J. Korte, Manager, Nuclear Security
J. Plona, Engineering Director
J. Plona, Engineering Director
NRCC. Lipa, Chief, Division of Reactor Projects, Branch 4  
NRC
Attachment
C. Lipa, Chief, Division of Reactor Projects, Branch 4
2LIST OF ITEMS OPENED, CLOSED, AND DISCUSSED
                                                1      Attachment
Opened05000341/2006003-05URIInappropriate Use of Risk in Operability Evaluations(Section 1R15.3)Opened and Closed05000341/2006003-01NCVUnauthorized Transient Combustibles in Safety-RelatedAreas (Section 1R05.2)05000341/2006003-02NCVImproper Storage of Chemicals Affecting Fire FightingResponse (Section 1R05.3)05000341/2006003-03NCVInadequate Maintenance Risk Assessment(Section 1R13.2)05000341/2006003-04NCVImproper Evaluation of Standby Liquid Control OperabilityDuring Tank Sparging (Section 1R15.2)05000341/2006003-06NCVInadequate Controls for Venting the Reactor PressureVessel Head (Section 1R20.1)Closed05000341/2006-001LERExcessive Feedwater Check Valve Leakage at ContainmentPenetrationDiscussedNone.  
 
Attachment
                LIST OF ITEMS OPENED, CLOSED, AND DISCUSSED
3LIST OF DOCUMENTS REVIEWEDThe following is a list of documents reviewed during the inspection. Inclusion on this list doesnot imply that the NRC inspectors reviewed the documents in their entirety but rather that
Opened
05000341/2006003-05  URI  Inappropriate Use of Risk in Operability Evaluations
                            (Section 1R15.3)
Opened and Closed
05000341/2006003-01  NCV  Unauthorized Transient Combustibles in Safety-Related
                            Areas (Section 1R05.2)
05000341/2006003-02  NCV  Improper Storage of Chemicals Affecting Fire Fighting
                            Response (Section 1R05.3)
05000341/2006003-03  NCV  Inadequate Maintenance Risk Assessment
                            (Section 1R13.2)
05000341/2006003-04  NCV  Improper Evaluation of Standby Liquid Control Operability
                            During Tank Sparging (Section 1R15.2)
05000341/2006003-06  NCV  Inadequate Controls for Venting the Reactor Pressure
                            Vessel Head (Section 1R20.1)
Closed
05000341/2006-001    LER  Excessive Feedwater Check Valve Leakage at Containment
                            Penetration
Discussed
None.
                                        2                                    Attachment
 
                                LIST OF DOCUMENTS REVIEWED
The following is a list of documents reviewed during the inspection. Inclusion on this list does
not imply that the NRC inspectors reviewed the documents in their entirety but rather that
selected sections of portions of the documents were evaluated as part of the overall inspection
selected sections of portions of the documents were evaluated as part of the overall inspection
effort. Inclusion of a document on this list does not imply NRC acceptance of the document orany part of it, unless this is stated in the body of the inspection report.1R01:Adverse Weather ProtectionCARD 06-23861, 06/05/06; Procedure Enhancement for TBHVAC (NRC Comment)Procedure 27.000.06, Rev 0, 02/27/03; Performance Evaluation Procedure, Hot WeatherOperations
effort. Inclusion of a document on this list does not imply NRC acceptance of the document or
Open/Closed Work Requests by Related Work Code; 05/04/061R04:Equipment AlignmentDrawing 6M721-5706-3, 2/16/00; RHR Service Water Make Up Decant and Overflow SystemsFunctional Operating Sketch
any part of it, unless this is stated in the body of the inspection report.
Drawing 6M721-5706-1, 3/5/04; Residual Heat Removal (RHR) Division II Functional OperatingSketch
1R01: Adverse Weather Protection
03-00120, 01/02/03; Pinhole leak in piping  
CARD 06-23861, 06/05/06; Procedure Enhancement for TBHVAC (NRC Comment)
03-13694, 6/17/03; Document the Condition of General Service Water Piping04-24918, 10/25/04; P4100F402A installed at the bottom of the pipe06-11615, 05/19/06; EDG Electrical Lineup Load Description Changes
Procedure 27.000.06, Rev 0, 02/27/03; Performance Evaluation Procedure, Hot Weather
06-21618, 03/28/06; E1100F050A Failed PI Leak Test SR 3.4.5.106-22730, 4/24/06; NRC-Identified Concerns in GSW Pumphouse06-23447, 05/18/06; 23.205 Att 1B enhancement
Operations
06-23494, 05/20/06; E1100F050A actuator failed to open valve23.131, Rev.86; General Service Water System
Open/Closed Work Requests by Related Work Code; 05/04/06
1R04: Equipment Alignment
Drawing 6M721-5706-3, 2/16/00; RHR Service Water Make Up Decant and Overflow Systems
Functional Operating Sketch
Drawing 6M721-5706-1, 3/5/04; Residual Heat Removal (RHR) Division II Functional Operating
Sketch
03-00120, 01/02/03; Pinhole leak in piping
03-13694, 6/17/03; Document the Condition of General Service Water Piping
04-24918, 10/25/04; P4100F402A installed at the bottom of the pipe
06-11615, 05/19/06; EDG Electrical Lineup Load Description Changes
06-21618, 03/28/06; E1100F050A Failed PI Leak Test SR 3.4.5.1
06-22730, 4/24/06; NRC-Identified Concerns in GSW Pumphouse
06-23447, 05/18/06; 23.205 Att 1B enhancement
06-23494, 05/20/06; E1100F050A actuator failed to open valve
23.131, Rev.86; General Service Water System
43.000.005, Rev. 30; Visual Examination of Piping and Components (VT-2)
43.000.005, Rev. 30; Visual Examination of Piping and Components (VT-2)
23.208, Rev. 81; RHR Complex Service Water Systems23.205, Rev. 94; Residual Heat Removal System1R05:Fire ProtectionCARD 06-23365; Door is not latching; Dated May 15, 2006 (NRC-Identified)CARD 06-23388; Transient Combustibles in the RHR; Dated May 16, 2006 (NRC-Identified)MOP11; Fire Protection; Revision 10
23.208, Rev. 81; RHR Complex Service Water Systems
Fire Brigade Drill Scenario 6, Rev. 11/29/94; First Floor Radioactive Waste Chemical LabStorage Area
23.205, Rev. 94; Residual Heat Removal System
Fire protection Pre-Plan FP-RDWST, Rev. 4; Radwaste Building Zones 22, 23, 24, and 251R06:Flood Protection MeasuresCARD 06-21354; High Pressure Coolant Injection Room Flooded due to Drains backing Up;
1R05: Fire Protection
CARD 06-23365; Door is not latching; Dated May 15, 2006 (NRC-Identified)
CARD 06-23388; Transient Combustibles in the RHR; Dated May 16, 2006 (NRC-Identified)
MOP11; Fire Protection; Revision 10
Fire Brigade Drill Scenario 6, Rev. 11/29/94; First Floor Radioactive Waste Chemical Lab
Storage Area
Fire protection Pre-Plan FP-RDWST, Rev. 4; Radwaste Building Zones 22, 23, 24, and 25
1R06: Flood Protection Measures
CARD 06-21354; High Pressure Coolant Injection Room Flooded due to Drains backing Up;
3/18/06
3/18/06
CARD 06-22600; Moderate Energy Line Break Evaluation; 4/21/06 (NRC-Identified)  
CARD 06-22600; Moderate Energy Line Break Evaluation; 4/21/06 (NRC-Identified)
Attachment
                                                  3                                Attachment
4Nuclear Generation Memo TMPE-94-0308; May 18, 1994; Flood Protection Review6M721-2223, Rev U, 11/24/06; Diagram Equipment Drains All Floors Auxiliary and ReactorBuildings
 
6M721-2224, Rev W, 11/24/04; Diagram Floor Drains All Floors Auxiliary and Reactor Buildings6M721-2032, Rev BO, 04/19/06; Sump Pump Diagram Radwaste System
Nuclear Generation Memo TMPE-94-0308; May 18, 1994; Flood Protection Review
6M721-2032-1, Rev AI, 04/19/06; Sump Pump Diagram Radwaste System1R07:Heat Sink PerformanceWR TG25060421; Perform RHR Division II Heat Exchanger Performance Test; 3/22/061R11:Licensed Operator RequalificationScenario SS-OP-802-3300, Rev. 0; Anticipated Transient Without Scram with Small SteamLeak; 1/26/061R12:Maintenance EffectivenessDesign Specification 3071-128-EZ-06; Electrical Design Instructions Molded Case CircuitBreakers
6M721-2223, Rev U, 11/24/06; Diagram Equipment Drains All Floors Auxiliary and Reactor
Buildings
6M721-2224, Rev W, 11/24/04; Diagram Floor Drains All Floors Auxiliary and Reactor Buildings
6M721-2032, Rev BO, 04/19/06; Sump Pump Diagram Radwaste System
6M721-2032-1, Rev AI, 04/19/06; Sump Pump Diagram Radwaste System
1R07: Heat Sink Performance
WR TG25060421; Perform RHR Division II Heat Exchanger Performance Test; 3/22/06
1R11: Licensed Operator Requalification
Scenario SS-OP-802-3300, Rev. 0; Anticipated Transient Without Scram with Small Steam
Leak; 1/26/06
1R12: Maintenance Effectiveness
Design Specification 3071-128-EZ-06; Electrical Design Instructions Molded Case Circuit
Breakers
Maintenance Rule Conduct Manual MMR, Appendix E, Rev 4; Maintenance Rule SSC Specific
Maintenance Rule Conduct Manual MMR, Appendix E, Rev 4; Maintenance Rule SSC Specific
Functions
Functions
Line 667: Line 1,541:
CARD 97-10182, 10/27/97; Defective Molded Case Circuit Breaker
CARD 97-10182, 10/27/97; Defective Molded Case Circuit Breaker
CARD 03-01098,05/30/03; Reactor Protection System - Function Failure
CARD 03-01098,05/30/03; Reactor Protection System - Function Failure
03-19510,07/20/03; Safety Eval 95-0002 is Used as an Operability Evaluation for LPCI with theRHR Minimum Flow Valves Open
03-19510,07/20/03; Safety Eval 95-0002 is Used as an Operability Evaluation for LPCI with the
RHR Minimum Flow Valves Open
CARD 04-22685, 07/02/04; Generator Transformer - Function Failure
CARD 04-22685, 07/02/04; Generator Transformer - Function Failure
CARD 04-23307. 08/03/04; Motor Control Centers & Dist. Cabinets
CARD 04-23307. 08/03/04; Motor Control Centers & Dist. Cabinets
CARD 05-23490, 06/21/05; Auxiliary Electrical - Function FailureCARD 06-21363, 04-02-06; Auxiliary Electrical - Function FailureCARD 06-21527, 04/09/06; Residual Heat Removal System - Function Failure
CARD 05-23490, 06/21/05; Auxiliary Electrical - Function Failure
CARD 06-21363, 04-02-06; Auxiliary Electrical - Function Failure
CARD 06-21527, 04/09/06; Residual Heat Removal System - Function Failure
CARD 06-22270, 04/12/06, Maintenance Rule Function T4100-09 should be included in
CARD 06-22270, 04/12/06, Maintenance Rule Function T4100-09 should be included in
Maintenance Rule Scope Investigation
Maintenance Rule Scope Investigation
Procedure 35.306.008, Rev 46; Maintenance Procedure, ITE Gould Motor Control Center LoadCompartment
Procedure 35.306.008, Rev 46; Maintenance Procedure, ITE Gould Motor Control Center Load
Procedure 35.306.018, Rev 5; Maintenance Procedure, Spectrum Technology Motor ControlCenter Load Compartment1R13:Maintenance Risk Assessment and Emergent Work EvaluationFermi 2 Daily Plant Status, April 2, 2006Scheduler's Evaluation for Fermi 2, April 2, 2006
Compartment
Procedure 35.306.018, Rev 5; Maintenance Procedure, Spectrum Technology Motor Control
Center Load Compartment
1R13: Maintenance Risk Assessment and Emergent Work Evaluation
Fermi 2 Daily Plant Status, April 2, 2006
Schedulers Evaluation for Fermi 2, April 2, 2006
Fermi 2 Daily Plant Status, April 17, 2006
Fermi 2 Daily Plant Status, April 17, 2006
Scheduler's Evaluation for Fermi 2, April 17, 2006  
Schedulers Evaluation for Fermi 2, April 17, 2006
Attachment
                                                4                                Attachment
5Fermi 2 Daily Plant Status, April 30, 2006Scheduler's Evaluation for Fermi 2, April 30, 2006
 
Fermi 2 Daily Plant Status, April 30, 2006
Schedulers Evaluation for Fermi 2, April 30, 2006
Fermi 2 Daily Plant Status, June 26, 2006
Fermi 2 Daily Plant Status, June 26, 2006
Scheduler's Evaluation for Fermi 2, June 26, 2006
Schedulers Evaluation for Fermi 2, June 26, 2006
CARD 06-21892, 4/4/06; NRC Questions related to Temporary Cooling Installed for Division IBattery Test (NRC-Identified)CARD 06-24495, 7/7/06; Work Risk Assessment and Temporary Equipment Controls(NRC-Identified)WR 0219060414; Perform 42.309.05 Division I (5 Year) 130/260 VDC batter Check (2A-1 Only)
CARD 06-21892, 4/4/06; NRC Questions related to Temporary Cooling Installed for Division I
WR 1219060414; Perform 42.309.05 Division I (5 Year) 130/260 VDC batter Check (2A-2 Only)1R14:Non-Routine EventsCARD 06-24113; Main Steam Bypass Valves Opened Unintentionally During Power Ascension;
Battery Test (NRC-Identified)
CARD 06-24495, 7/7/06; Work Risk Assessment and Temporary Equipment Controls
(NRC-Identified)
WR 0219060414; Perform 42.309.05 Division I (5 Year) 130/260 VDC batter Check (2A-1 Only)
WR 1219060414; Perform 42.309.05 Division I (5 Year) 130/260 VDC batter Check (2A-2 Only)
1R14: Non-Routine Events
CARD 06-24113; Main Steam Bypass Valves Opened Unintentionally During Power Ascension;
6/18/06
6/18/06
CARD 06-23588; Mode 5 Reactor SCRAM During Installation of SRM Shorting Links; 5/24/06
CARD 06-23588; Mode 5 Reactor SCRAM During Installation of SRM Shorting Links; 5/24/06
CARD 06-23501; Full In Light for Control Rod 50-27 on Full Core Display is Intermittent;
CARD 06-23501; Full In Light for Control Rod 50-27 on Full Core Display is Intermittent;
 
5/20/06
5/20/061R15:Operability EvaluationsDrawing - 5744, Rev. BK; Emergency Equipment Cooling Water Division I; 11/23/05WR 000Z060107; Remove and Reinstall Insulation on E1100F031B; 2/9/06
1R15: Operability Evaluations
Drawing - 5744, Rev. BK; Emergency Equipment Cooling Water Division I; 11/23/05
WR 000Z060107; Remove and Reinstall Insulation on E1100F031B; 2/9/06
WR 000Z062027; Replace Contaminated Insulation; 6/12/06
WR 000Z062027; Replace Contaminated Insulation; 6/12/06
CARD 06-24156; Affects of Accidents not Addressed in Insulation Removal Evaluation for
CARD 06-24156; Affects of Accidents not Addressed in Insulation Removal Evaluation for
E1100F031B; 6/20/06 (NRC Identified)CARD 01-17302; There are no Site Guidelines for Insulation Removal on Operable Equipment;
E1100F031B; 6/20/06 (NRC Identified)
 
CARD 01-17302; There are no Site Guidelines for Insulation Removal on Operable Equipment;
8/14/01
8/14/01
CARD 06-23898; EECW M/U Pump IST Flow Unattainable; 6/7/06
CARD 06-23898; EECW M/U Pump IST Flow Unattainable; 6/7/06
Line 698: Line 1,590:
CARD 05-21940; Engineering Evaluation for On-Line Insulation Removal; 3/23/05
CARD 05-21940; Engineering Evaluation for On-Line Insulation Removal; 3/23/05
CARD 06-23913; Replace Contaminated Insulation; 6/8/06
CARD 06-23913; Replace Contaminated Insulation; 6/8/06
CARD 06-23785; Standby Liquid Control Operability During Sparging Activities; 6/1/06 (NRC-Identified)
CARD 06-23785; Standby Liquid Control Operability During Sparging Activities; 6/1/06 (NRC-
CARD 99-13240; Inoperability of Standby Liquid Control During Air Sparging; 4/15/991R19:Post-Maintenance TestingEDP - 31880 120 KV Switchyard Upgrade Engineering Change Request 33690-1, Rev A, 03/14/06; Replacement of Drywell Cooler CoilsT470B003 and T4700B004
Identified)
Equivalent Replacement Evaluation (ERE) 34173, Rev 0, 04/18/06; E1150F608 MOV MotorReplacement
CARD 99-13240; Inoperability of Standby Liquid Control During Air Sparging; 4/15/99
Oil Sample Analysis Reports for C1106C001A, "E" Control Rod Drive Pump; 01/01/06 -
1R19: Post-Maintenance Testing
 
EDP - 31880 120 KV Switchyard Upgrade
Engineering Change Request 33690-1, Rev A, 03/14/06; Replacement of Drywell Cooler Coils
T470B003 and T4700B004
Equivalent Replacement Evaluation (ERE) 34173, Rev 0, 04/18/06; E1150F608 MOV Motor
Replacement
Oil Sample Analysis Reports for C1106C001A, E Control Rod Drive Pump; 01/01/06 -
06/29/06
06/29/06
CARD 06-22258, 04/12/06; CTG equipment issues discovered during IPTE 04-02
CARD 06-22258, 04/12/06; CTG equipment issues discovered during IPTE 04-02
CARD 06-22982, 4/30/06; Inboard MSIV A will not slow closeCARD 06-23031, 5/1/06; MSIV B2103F028B RPS Limit Switch did not actuate when expected  
CARD 06-22982, 4/30/06; Inboard MSIV A will not slow close
Attachment
CARD 06-23031, 5/1/06; MSIV B2103F028B RPS Limit Switch did not actuate when expected
6CARD 06-22634, 4/22/06; "A" Inboard MSIV limit switch, PIS B21N572A, will not change stateDrawing SD-F-0179, Rev. A, 9/25/05; Diagram Line Breaker Control 120KV, POS GKDrawing SD-2500-01, Rev. A, 2/28/06; One Line Diagram Plant 4160V & 480VDrawing SD-2500-02, Rev. A, 2/23/06; One Line Diagram 13.8KVDrawing SD-F-0001, Rev. A, 2.23/06; One Line Diagram 120 KV Switchyard
                                                5                                  Attachment
 
CARD 06-22634, 4/22/06; A Inboard MSIV limit switch, PIS B21N572A, will not change state
Drawing SD-F-0179, Rev. A, 9/25/05; Diagram Line Breaker Control 120KV, POS GK
Drawing SD-2500-01, Rev. A, 2/28/06; One Line Diagram Plant 4160V & 480V
Drawing SD-2500-02, Rev. A, 2/23/06; One Line Diagram 13.8KV
Drawing SD-F-0001, Rev. A, 2.23/06; One Line Diagram 120 KV Switchyard
IPTE 04-02, 120KV Switchyard Upgrade
IPTE 04-02, 120KV Switchyard Upgrade
Procedure 24.137.01, Rev. 34; Main Steam Isolation Channel Functional Test
Procedure 24.137.01, Rev. 34; Main Steam Isolation Channel Functional Test
24.206.01, Rev 63, 05/08/06; RCIC System Pump and Valve Operability Test43.000.005, Rev 30, 03/22/06; Visual Examination of Piping and Components (VT-2)43.401.303, Rev 32, 10/24/05; Local Leakage Rate Testing for Penetration X-9AWR B203040100, 04/10/06; B2100F010A - Nuclear Boiler Feedwater Supply Inboard PrimaryContainment Check Valve
24.206.01, Rev 63, 05/08/06; RCIC System Pump and Valve Operability Test
WR 000Z050487, 04/29/06;B3105F031A - Reactor Recirculation Pump "A" Discharge Valve
43.000.005, Rev 30, 03/22/06; Visual Examination of Piping and Components (VT-2)
WR T210040100, 04/10/06; B2100F076A - Nuclear Boiler Feedwater Supply Check ValveWR 000Z052131, 04/19/06; Inservice Testing, Drywell Cooler #4
43.401.303, Rev 32, 10/24/05; Local Leakage Rate Testing for Penetration X-9A
WR 000Z060156, 6/19/06; "E" Control Rod Drive Inboard Pump Bearing Oil level Bulls eye Dirty1R20:Refueling and Outage ActivitiesApparent Cause Determination for Damage Found in the Main Generator During RF11 RobotInspections CARD 06-21922
WR B203040100, 04/10/06; B2100F010A - Nuclear Boiler Feedwater Supply Inboard Primary
Inspection Requirement Form, Requisition Number: 9086929; 04/19/2006
Containment Check Valve
WR 000Z050487, 04/29/06;B3105F031A - Reactor Recirculation Pump A Discharge Valve
WR T210040100, 04/10/06; B2100F076A - Nuclear Boiler Feedwater Supply Check Valve
WR 000Z052131, 04/19/06; Inservice Testing, Drywell Cooler #4
WR 000Z060156, 6/19/06; E Control Rod Drive Inboard Pump Bearing Oil level Bulls eye Dirty
1R20: Refueling and Outage Activities
Apparent Cause Determination for Damage Found in the Main Generator During RF11 Robot
Inspections CARD 06-21922
Inspection Requirement Form, Requisition Number: 9086929; 04/19/2006
Drawing 6M721-3722, Rev A; Flow Diagram & Details of Purging Unit - Reactor Pressure
Drawing 6M721-3722, Rev A; Flow Diagram & Details of Purging Unit - Reactor Pressure
Vessel - Unit 2
Vessel - Unit 2
Safety Tagging Record 2006-002089
Safety Tagging Record 2006-002089
CARD 06-21534, 03/26/2006; Continuous Air Monitor Alarm on Refueling Floor
CARD 06-21534, 03/26/2006; Continuous Air Monitor Alarm on Refueling Floor
CARD 06-22590, 04/21/2006;  
CARD 06-22590, 04/21/2006; NRC identified concern with Div 1 Core Spray and Defense in
NRC identified concern with Div 1 Core Spray and Defense inDepth Investigation
Depth Investigation
CARD 06-22642, 04/22/2006; Are EDG Surveillance's Testing What They Are Setup to TestCARD 06-22667, 04/23/2006; RPV Venting Unit Configuration Control DiscrepanciesCARD 06-23114, 05/03/2006; NRC Concern: Review of ERE-34173 "E1150F608 MOV MotorReplacement
CARD 06-22642, 04/22/2006; Are EDG Surveillances Testing What They Are Setup to Test
CARD 06-23793, 06/02/2006; NRC Concern - Material Released Without the Requirements ofEED Being Verified
CARD 06-22667, 04/23/2006; RPV Venting Unit Configuration Control Discrepancies
Procedure 24.106.06, Rev 25; Surveillance Procedure, SCRAM Discharge Volume Vent andDrain Valves SCRAM Operability Test
CARD 06-23114, 05/03/2006; NRC Concern: Review of ERE-34173 E1150F608 MOV Motor
Procedure 32.000.07, Rev 33; Crane Operation Procedure, Reactor Building Crane OperationProcedure 35.717.001, Rev 29; Maintenance Procedure, Reactor Building Crane - QuarterlyPreventive Maintenance
Replacement
Procedure 35.717.003, Rev 3; Maintenance Procedure, Reactor Building Crane - Annual PMInspection
CARD 06-23793, 06/02/2006; NRC Concern - Material Released Without the Requirements of
Procedure 43.401.303, Rev 32; Surveillance Procedure, Local Leakage Rate Testing forPenetration X-9A
EED Being Verified
Procedure 24.106.06, Rev 25; Surveillance Procedure, SCRAM Discharge Volume Vent and
Drain Valves SCRAM Operability Test
Procedure 32.000.07, Rev 33; Crane Operation Procedure, Reactor Building Crane Operation
Procedure 35.717.001, Rev 29; Maintenance Procedure, Reactor Building Crane - Quarterly
Preventive Maintenance
Procedure 35.717.003, Rev 3; Maintenance Procedure, Reactor Building Crane - Annual PM
Inspection
Procedure 43.401.303, Rev 32; Surveillance Procedure, Local Leakage Rate Testing for
Penetration X-9A
Work Control Conduct Manual MWC13, Rev 0; Outage Nuclear Safety
Work Control Conduct Manual MWC13, Rev 0; Outage Nuclear Safety
Maintenance Conduct Manual MMA07, Rev 14; Hoisting, Rigging and Load Handling  
Maintenance Conduct Manual MMA07, Rev 14; Hoisting, Rigging and Load Handling
Attachment
                                            6                                  Attachment
71R22:Surveillance TestingDrawing 6M721-5703-1, Rev. Y; Control Rod Drive System Functional Operating SketchCARD 06-22739, 4/24/06; Acrid smell from EDG #13 local control cabinet
CARD 06-23031, 5/1/06; MSIV B2103F028B RPS Limit Switch did not actuate when expectedCARD 06-22653, 04/23/06; HCU 46-27 Conduit for wiring to accumulator pressure switchneeds repair
CARD 06-22999, 05/01/06; Enhancements to 24.405.03CARD 06-21681; Potential Enhancement for MSIV Switch Calibrations; 3/20/06 (NRC-Identified)
CARD 06-21720; NRC Question Regarding MSIV Switch Testing; 3/31/06 (NRC-Identified)CARD 06-22046; Loss of SLC Squib Valve "A" Continuity Light During Performance of


1R22: Surveillance Testing
Drawing 6M721-5703-1, Rev. Y; Control Rod Drive System Functional Operating Sketch
CARD 06-22739, 4/24/06; Acrid smell from EDG #13 local control cabinet
CARD 06-23031, 5/1/06; MSIV B2103F028B RPS Limit Switch did not actuate when expected
CARD 06-22653, 04/23/06; HCU 46-27 Conduit for wiring to accumulator pressure switch
needs repair
CARD 06-22999, 05/01/06; Enhancements to 24.405.03
CARD 06-21681; Potential Enhancement for MSIV Switch Calibrations; 3/20/06 (NRC-
Identified)
CARD 06-21720; NRC Question Regarding MSIV Switch Testing; 3/31/06 (NRC-Identified)
CARD 06-22046; Loss of SLC Squib Valve A Continuity Light During Performance of
24.139.03; 4/7/06
24.139.03; 4/7/06
Procedure 24.106.06, Rev 25; Surveillance Procedure, SCRAM Discharge Volume Vent andDrain Valves SCRAM Operability Test
Procedure 24.106.06, Rev 25; Surveillance Procedure, SCRAM Discharge Volume Vent and
Procedure 24.106.08, Rev. 3; CRD Hydraulic Unit Accumulator Integrity TestProcedure 24.137.01, Rev. 34; Main Steam Isolation Channel Functional Test
Drain Valves SCRAM Operability Test
Procedure 24.405.03, Rev. 33; Secondary Containment Operability TestProcedure 24.307.03, Rev. 38; EDG 13 - Loss of Offsite Power and ECCS Start with Loss of
Procedure 24.106.08, Rev. 3; CRD Hydraulic Unit Accumulator Integrity Test
Procedure 24.137.01, Rev. 34; Main Steam Isolation Channel Functional Test
Procedure 24.405.03, Rev. 33; Secondary Containment Operability Test
Procedure 24.307.03, Rev. 38; EDG 13 - Loss of Offsite Power and ECCS Start with Loss of
Offsite Power Test
Offsite Power Test
Procedure 24.202.02, Rev. 42; HPCI Flow Rate Test at 165 psig Reactor Steam Pressure
Procedure 24.202.02, Rev. 42; HPCI Flow Rate Test at 165 psig Reactor Steam Pressure
Procedure 24.206.04, Rev. 44; RCIC System Automatic Actuation and Flow Test
Procedure 24.206.04, Rev. 44; RCIC System Automatic Actuation and Flow Test
Procedure 43.401.500, Rev 34; Surveillance Procedure, Local Leakage Rate Testing forPenetration X-7A, X-7B, X-7C, and X-7D
Procedure 43.401.500, Rev 34; Surveillance Procedure, Local Leakage Rate Testing for
Procedure 43.401.500, Rev 35; Surveillance Procedure, Local Leakage Rate Testing forPenetration X-7A, X-7B, X-7C, and X-7D  
Penetration X-7A, X-7B, X-7C, and X-7D
Procedure 43.401.500, Rev 35; Surveillance Procedure, Local Leakage Rate Testing for
Penetration X-7A, X-7B, X-7C, and X-7D
Procedure 24.402.06; Rev. 32; Drywell to Suppression Chamber Bypass Leak Test
Procedure 24.402.06; Rev. 32; Drywell to Suppression Chamber Bypass Leak Test
Procedure 35.139.002; Rev. 27; SLC System Explosive Valve Insert Replacement
Procedure 35.139.002; Rev. 27; SLC System Explosive Valve Insert Replacement
Procedure 24.139.03, Rev. 40; SLC Manual Initiation, RWCU Isolation, and Storage tankHeater Operability Test
Procedure 24.139.03, Rev. 40; SLC Manual Initiation, RWCU Isolation, and Storage tank
Heater Operability Test
WR 0311060425; Perform 24.402.06 Drywell to Suppression Chamber Bypass Leak Test;
WR 0311060425; Perform 24.402.06 Drywell to Suppression Chamber Bypass Leak Test;
3/25/06
3/25/06
WR 0518041022; Perform 44.010.063 RPS MSIV Outboard Valve Limit Switch, Div. I and II,
WR 0518041022; Perform 44.010.063 RPS MSIV Outboard Valve Limit Switch, Div. I and II,
Calibration
Calibration
WR 1245060421; Perform 24.139.03 SLC Loop "B" Pump Flow, Manual Initiate, and Squib
WR 1245060421; Perform 24.139.03 SLC Loop B Pump Flow, Manual Initiate, and Squib
Firing; 4/21/06
Firing; 4/21/06
1EP6:Drill EvaluationScenario SS-OP-802-3300, Rev. 0; Anticipated Transient Without Scram with Small SteamLeak; 1/26/06
1EP6: Drill Evaluation
2OS1: Access Control to Radiologically Significant AreasCARD 05-26818; Primary Containment Atmosphere Sample Pump; T5001-C003 Will Not Start;dated December 5, 2005
Scenario SS-OP-802-3300, Rev. 0; Anticipated Transient Without Scram with Small Steam
Leak; 1/26/06
2OS1: Access Control to Radiologically Significant Areas
CARD 05-26818; Primary Containment Atmosphere Sample Pump; T5001-C003 Will Not Start;
dated December 5, 2005
CARD 06-11546; WGI Employee Felt Something in His Left Eye after Removing Protective
CARD 06-11546; WGI Employee Felt Something in His Left Eye after Removing Protective
Clothing at Drywell Step-off Pad; dated April 5, 2006
Clothing at Drywell Step-off Pad; dated April 5, 2006
CARD 06-21534; High Radiation Alarm on Refuel Floor; dated March 26, 2006  
CARD 06-21534; High Radiation Alarm on Refuel Floor; dated March 26, 2006
Attachment
                                                7                              Attachment
8CARD 06-21640; Unnecessary Contamination of Personnel; dated March 29, 2006CARD 06-21639; Evaluate Dose an Dose Rate Alarms for Fast Entry Electronic Dosimeters;
 
CARD 06-21640; Unnecessary Contamination of Personnel; dated March 29, 2006
CARD 06-21639; Evaluate Dose an Dose Rate Alarms for Fast Entry Electronic Dosimeters;
dated March 29, 2006
dated March 29, 2006
CARD 06-20962; Worker Electronic Dosimeter Alarm on Incorrect Task; dated February 23,
CARD 06-20962; Worker Electronic Dosimeter Alarm on Incorrect Task; dated February 23,
2006
2006
CARD 06-21177; Unexpected Dose Rate Alarm; dated March 8, 2006
CARD 06-21177; Unexpected Dose Rate Alarm; dated March 8, 2006
CARD 06-21787; Entering High Radiation Area on Incorrect Task; dated April 1, 2006
CARD 06-21787; Entering High Radiation Area on Incorrect Task; dated April 1, 2006
CARD 06-21807; Evaluate Reactor Building Ventilation Impact on the Spread of Contaminationduring RF11 Vessel Fill Up; dated April 2, 2006CARD 06-21857; Drywell Stepoff Pad Poor Radiation Protection Practices; dated April 3, 2006CARD 06-21873; Potential Release of Radioactive Contamination; dated April 4, 2006CARD 06- 21868; Workers Entered Top of Torus High Radiation Area on Wrong Radiation
CARD 06-21807; Evaluate Reactor Building Ventilation Impact on the Spread of Contamination
during RF11 Vessel Fill Up; dated April 2, 2006
CARD 06-21857; Drywell Stepoff Pad Poor Radiation Protection Practices; dated April 3, 2006
CARD 06-21873; Potential Release of Radioactive Contamination; dated April 4, 2006
CARD 06- 21868; Workers Entered Top of Torus High Radiation Area on Wrong Radiation
Work Permit; dated April 4, 2006
Work Permit; dated April 4, 2006
CARD 06-21944; Foreign Material Found Inside Main Condenser Upper Steam Space; dated
CARD 06-21944; Foreign Material Found Inside Main Condenser Upper Steam Space; dated
Line 773: Line 1,715:
EP-225; Radiological Medical Emergencies; Revision 13
EP-225; Radiological Medical Emergencies; Revision 13
RF11 ALARA Self-Assessment; dated April 4, 2006
RF11 ALARA Self-Assessment; dated April 4, 2006
2OS2As-Low-As-Is-Reasonably-Achievable Planning And Controls (ALARA)RWP 06-1110; In-Service Inspections; Revision 0RWP 06-1103; Install and Remove Temporary Shielding, Install Permanent Shielding;
2OS2 As-Low-As-Is-Reasonably-Achievable Planning And Controls (ALARA)
RWP 06-1110; In-Service Inspections; Revision 0
RWP 06-1103; Install and Remove Temporary Shielding, Install Permanent Shielding;
Revision 0
Revision 0
RWP 06-1105; Job Progress for Scaffold Activities in the Reactor Building Steam Tunnel and
RWP 06-1105; Job Progress for Scaffold Activities in the Reactor Building Steam Tunnel and
Line 780: Line 1,724:
RWP 06-1164; E1100F031A Cutout and Replace Check Valve; Revision 0
RWP 06-1164; E1100F031A Cutout and Replace Check Valve; Revision 0
RWP 06-1251; Perform Refuel Activities on Reactor Building 5; Revision 0
RWP 06-1251; Perform Refuel Activities on Reactor Building 5; Revision 0
CARD 06-21765; Work Initiated Without Radiation Protection Review; dated April 1, 2006CARD 06-21911; E100F031A Glovebag Not Installed Properly; dated April 5, 2006
CARD 06-21765; Work Initiated Without Radiation Protection Review; dated April 1, 2006
CARD 06-21911; E100F031A Glovebag Not Installed Properly; dated April 5, 2006
CARD 06-21947; E1100F060A Re-pack Extra Time and Dose Above Initial Estimate; dated
CARD 06-21947; E1100F060A Re-pack Extra Time and Dose Above Initial Estimate; dated
April 5, 2006
April 5, 2006
Procedure 63.000.100; Respirator Evaluation Work Sheet (RWP 06-1117); Revision 04OA2:Identification and Resolution of ProblemsCARDs initiated between 1/1/06 and 06/30/06
Procedure 63.000.100; Respirator Evaluation Work Sheet (RWP 06-1117); Revision 0
4OA3:Event Followup (71153)NRC-06-0037 Letter; Licensee Event report No. 2006-001, "Excessive Feedwater Check ValveLeakage At Containment Penetration;" dated May 24, 20064OA7Licensee-Identified ViolationsCARD 06-21389; Failure to Perform Required Surveys in Accordance withProcedure 67.000.102; dated March 21, 2006
4OA2: Identification and Resolution of Problems
CARDs initiated between 1/1/06 and 06/30/06
4OA3: Event Followup (71153)
NRC-06-0037 Letter; Licensee Event report No. 2006-001, Excessive Feedwater Check Valve
Leakage At Containment Penetration; dated May 24, 2006
4OA7 Licensee-Identified Violations
CARD 06-21389; Failure to Perform Required Surveys in Accordance with
Procedure 67.000.102; dated March 21, 2006
Procedure 67.000.103; Survey of Outgoing Radioactive Material Shipments; Revision 16
Procedure 67.000.103; Survey of Outgoing Radioactive Material Shipments; Revision 16
Procedure 67.000.102; Survey of Incoming Radioactive Material Shipments; Revision 0  
Procedure 67.000.102; Survey of Incoming Radioactive Material Shipments; Revision 0
Attachment
                                              8                                Attachment
9LIST OF ACRONYMS USEDALARAAs Low As Reasonable AchievableCARDCondition Assessment Resolution Document
 
CDFCore Damage Frequency
                        LIST OF ACRONYMS USED
CFRCode of Federal Regulations
ALARA As Low As Reasonable Achievable
CTGCombustion Turbine Generator
CARD  Condition Assessment Resolution Document
DRPDivision of Reactor Projects
CDF  Core Damage Frequency
EDGEmergency Diesel Generator
CFR  Code of Federal Regulations
GSWGeneral Service Water
CTG  Combustion Turbine Generator
HPCIHigh Pressure Coolant Injection
DRP  Division of Reactor Projects
IMCInspection Manual Chapter
EDG  Emergency Diesel Generator
LERLicensee Event Report
GSW  General Service Water
LERFLarge Early Release Frequency
HPCI  High Pressure Coolant Injection
LLRTLocal Leak Rate Test
IMC  Inspection Manual Chapter
MCCMotor Control Center
LER  Licensee Event Report
MSIVMain Steam Isolation Valve
LERF  Large Early Release Frequency
NCVNon-Cited Violation
LLRT  Local Leak Rate Test
NRCNuclear Regulatory Commission
MCC  Motor Control Center
PIPerformance Indicator
MSIV  Main Steam Isolation Valve
PMTPost-Maintenance Testing
NCV  Non-Cited Violation
RCICReactor Core Isolation Cooling
NRC  Nuclear Regulatory Commission
RCSReactor Coolant System
PI    Performance Indicator
RHRResidual Heat Removal
PMT  Post-Maintenance Testing
RHRSWResidual Heat Removal Service WaterRPSReactor Protection System  
RCIC  Reactor Core Isolation Cooling
RPSMGReactor Protection System Motor Generator
RCS  Reactor Coolant System
RPTRadiation Protection Technician
RHR  Residual Heat Removal
RWCUReactor Water Cleanup  
RHRSW Residual Heat Removal Service Water
RWPRadiation Work Package
RPS  Reactor Protection System
SCFHStandard Cubic Feet Per Hour  
RPSMG Reactor Protection System Motor Generator
SCFMStandard Cubic Feet Per Minute
RPT  Radiation Protection Technician
SDPSignificance Determination Process
RWCU  Reactor Water Cleanup
SGTSStandby Gas Treatment System
RWP  Radiation Work Package
SLCStandby Liquid Control
SCFH  Standard Cubic Feet Per Hour
SPARStandardized Plant Analysis Risk
SCFM  Standard Cubic Feet Per Minute
SRASenior Reactor Analyst
SDP  Significance Determination Process
TMTemporary Modifications
SGTS  Standby Gas Treatment System
TSTechnical Specifications
SLC  Standby Liquid Control
UFSARUpdated Final Safety Analysis Report
SPAR  Standardized Plant Analysis Risk
WRWork Request
SRA  Senior Reactor Analyst
TM    Temporary Modifications
TS    Technical Specifications
UFSAR Updated Final Safety Analysis Report
WR    Work Request
                                      9        Attachment
}}
}}

Revision as of 15:28, 23 November 2019

IR 05000341-06-003; 04/01/2006-06/30/2006; Fermi Power Plant, Unit 2; Fire Protection, Maintenance Risk Assessment, Operability Evaluations, Refueling and Outage Activities
ML062160540
Person / Time
Site: Fermi DTE Energy icon.png
Issue date: 08/02/2006
From: Christine Lipa
NRC/RGN-III/DRP/RPB4
To: Cobb D
Detroit Edison
References
IR-06-003
Download: ML062160540 (48)


See also: IR 05000341/2006003

Text

August 2, 2006

Mr. Donald K. Cobb

Assistant Vice President

Nuclear Generation

Detroit Edison Company

6400 North Dixie Highway

Newport, MI 48166

SUBJECT: FERMI POWER PLANT, UNIT 2, NRC INTEGRATED

INSPECTION REPORT 05000341/2006003

Dear Mr. Cobb:

On June 30, 2006, the U.S. Nuclear Regulatory Commission (NRC) completed an integrated

inspection at your Fermi Power Plant, Unit 2. The enclosed report documents the inspection

findings which were discussed on July 11, 2006, with you and other members of your staff.

The inspection examined activities conducted under your license as they relate to safety and to

compliance with the Commissions rules and regulations and with the conditions of your license.

The inspectors reviewed selected procedures and records, observed activities, and interviewed

personnel.

Based on the results of this inspection, five findings of very low safety significance were

identified, all of which involved violations of NRC requirements. However, because these

findings were of very low safety significance and because the issues were entered into your

corrective program, the NRC is treating these findings as Non-Cited Violations in accordance

with Section VI.A.1 of the NRCs Enforcement Policy. If you contest the subject or severity of

a Non-Cited Violation, you should provide a response within 30 days of the date of this

inspection report, with the basis for your denial, to the U.S. Nuclear Regulatory Commission,

ATTN: Document Control Desk, Washington, DC 20555-0001, with a copy to the Regional

Administrator, U.S. Nuclear Regulatory Commission - Region III, 2443 Warrenville Road,

Suite 210, Lisle, IL 60532-4352; the Director, Office of Enforcement, U.S. Nuclear Regulatory

Commission, Washington, DC 20555-0001; and the Resident Inspector Office at the Fermi 2

facility.

In accordance with 10 CFR 2.390 of the NRCs Rules of Practice, a copy of this letter and

its enclosure will be made available electronically for public inspection in the NRC Public

D. Cobb -2-

Document Room or from the Publicly Available Records (PARS) component of NRCs

document system (ADAMS). ADAMS is accessible from the NRC Web site at

http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room).

Sincerely,

/RA/

Christine A. Lipa, Chief

Branch 4

Division of Reactor Projects

Docket No. 50-341

License No. NPF-43

Enclosure: Inspection Report 05000341/2006003

w/Attachment: Supplemental Information

cc w/encl: K. Hlavaty, Plant Manager

R. Gaston, Manager, Nuclear Licensing

D. Pettinari, Legal Department

Michigan Department of Environmental Quality

Waste and Hazardous Materials Division

M. Yudasz, Jr., Director, Monroe County

Emergency Management Division

Supervisor - Electric Operators

State Liaison Officer, State of Michigan

Wayne County Emergency Management Division

D. Cobb -2-

Document Room or from the Publicly Available Records (PARS) component of NRCs

document system (ADAMS). ADAMS is accessible from the NRC Web site at

http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room).

Sincerely,

Christine A. Lipa, Chief

Branch 4

Division of Reactor Projects

Docket No. 50-341

License No. NPF-43

Enclosure: Inspection Report 05000341/2006003

w/Attachment: Supplemental Information

cc w/encl: K. Hlavaty, Plant Manager

R. Gaston, Manager, Nuclear Licensing

D. Pettinari, Legal Department

Michigan Department of Environmental Quality

Waste and Hazardous Materials Division

M. Yudasz, Jr., Director, Monroe County

Emergency Management Division

Supervisor - Electric Operators

State Liaison Officer, State of Michigan

Wayne County Emergency Management Division

DOCUMENT NAME:E:\Filenet\ML062160540.wpd

G Publicly Available G Non-Publicly Available G Sensitive G Non-Sensitive

To receive a copy of this document, indicate in the concurrence box "C" = Copy without attach/encl "E" = Copy with attach/encl "N" = No copy

OFFICE RIII RIII

NAME RLerch:dtp CLipa

DATE 08/02/06 08/02/06

OFFICIAL RECORD COPY

Donald K. Cobb -3-

ADAMS Distribution:

LXR1

DHJ

RidsNrrDirsIrib

GEG

KGO

RMM3

CAA1

LSL (electronic IRs only)

C. Pederson, DRS (hard copy - IRs only)

DRPIII

DRSIII

PLB1

TXN

ROPreports@nrc.gov (inspection reports, final SDP letters, any letter with an IR number)

U. S. NUCLEAR REGULATORY COMMISSION

REGION III

Docket No: 50-341

License No: NPF-43

Report No: 05000341/2006003

Licensee: Detroit Edison Company

Facility: Fermi Power Plant, Unit 2

Location: Newport, Michigan

Dates: April 1 through June 30, 2006

Inspectors: R. Michael Morris, Senior Resident Inspector

T. Steadham, Resident Inspector

A. Wilson, NRC Headquarters

M. Franke, Senior Resident Inspector, Perry

M. Jordan, NRC Consultant

R. Langstaff, Senior Reactor Inspector

M. Mitchell, Radiation Specialist

Approved by: C. Lipa, Chief

Branch 4

Division of Reactor Projects

Enclosure

SUMMARY OF FINDINGS

IR 05000341/2006003; 04/01/2006-06/30/2006; Fermi Power Plant, Unit 2; Fire Protection,

Maintenance Risk Assessment, Operability Evaluations, Refueling and Outage Activities.

This report covers a 3-month period of inspection by resident inspectors and announced

baseline inspections by a regional radiation specialist inspector. Five Green findings, all of

which were associated with non-cited violations (NCVs) were identified. The significance of

most findings is indicated by their color (Green, White, Yellow, Red) using Inspection

Manual Chapter 0609, Significance Determination Process (SDP). Findings for which the

SDP does not apply may be Green after NRC management review. The NRCs program for

overseeing the safe operation of commercial nuclear power reactors is described in

NUREG-1649, Reactor Oversight Process, Revision 3, dated July 2000.

A. NRC-Identified and Self-Revealed Findings

Cornerstone: Initiating Events

perform an adequate risk assessment for the Division I battery load test. The licensee

failed to consider the effect the test would have on the temperature in the reactor

protection system motor generator set rooms. Consequently, the load bank used for the

test caused the room temperature to increase which necessitated the unanticipated

installation of a temporary fan to cool the room. The licensee entered this issue into

their corrective action program to evaluate any programmatic or procedural deficiencies

that may have contributed to this event.

This finding is more than minor because the licensees risk assessment failed to

consider maintenance activities that could increase the likelihood of an initiating event,

specifically a loss of shutdown cooling from a reactor protection system motor generator

set trip on high temperature. The finding is of very low safety significance because it did

not affect the ability of operators to recover from a loss of shutdown cooling if it had

occurred. The cause of the finding is related to the cross-cutting element of Human

Performance. (Section 1R13.2)

Cornerstone: Mitigating Systems

  • Green. The inspectors identified an NCV of license condition 2.C(9) due to the

presence of unauthorized transient combustible materials in the residual heat removal

complex. An office chair and a plastic trash bin half filled with paper were secured next

to the electrical panel and associated cable raceway for emergency diesel generator 12

ventilation in the emergency diesel generator 12 switchgear room. The licensee entered

this issue into their corrective action program and removed the unauthorized transient

combustible materials from the residual heat removal complex.

This finding is more than minor because it affected the Mitigating Systems Cornerstone

attribute for protection against external factors. Specifically, a fire involving the

unauthorized transient combustibles could have affected a nearby electrical panel and

associated cable raceway containing mitigating system equipment important to safety.

2 Enclosure

The finding is of very low safety significance because the unauthorized transient

combustible materials would not have ignited from existing sources of heat or electrical

energy. The cause of the finding is related to the cross-cutting element of Problem

Identification and Resolution. (Section 1R05.2)

Amendment 38, for the standby liquid control (SLC) system being inoperable for longer

than the allowed time without the plant being placed in hot shutdown. The licensee

failed to properly evaluate the operability of SLC during sparging activities when the

issue was raised in 1999. As a result, the licensee initiated a 21-hour sparge on the

SLC tank on August 24, 1999, and failed to take actions in accordance with the

Technical Specifications. After the deficient evaluation was identified on June 1, 2006,

the licensee revised the applicable procedures to declare the SLC system inoperable

during sparging the SLC tank. The licensee entered this issue into their corrective

action program.

This finding is more than minor because it represented a programmatic deficiency in the

licensees chemical control program which affected the ability of the fire brigade to

respond to and mitigate the effects of a fire. Upon management review, the finding is of

very low safety significance because the quantities of the relevant chemicals were low

and the storage location was sufficiently remote from mitigating equipment.

(Section 1R05.3)

Cornerstone: Emergency Preparedness

  • Green. The inspectors identified an NCV of license condition 2.C(9), for the failure to

appropriately store chemicals in accordance with the fire hazards analysis. The licensee

failed to evaluate the fire fighting response guidelines in NFPA-49 for various chemicals

brought into the protective area and, therefore, failed to appropriately store them as

required by the licensees fire hazards analysis. As a result, five normally stored

chemicals in the building have recommended fire fighting strategies that are inconsistent

with the licensees approved fire protection pre-plan. The licensee entered this issue

into their correction action program.

This finding is more than minor because it affected the equipment performance attribute

of the reactor safety cornerstone objective of ensuring the availability, reliability, and

capability of mitigating equipment to respond to initiating events to prevent undesirable

consequences. The finding is of very low safety significance because the total time of

sparging activities was short. (Section 1R15.2)

Cornerstone: Occupational Radiation Safety

  • Green. A self-revealed NCV was identified for the licensees failure to comply with

Technical Specification 5.4.1.a, written procedures shall be established, implemented,

and maintained covering applicable procedures recommended in Regulatory

Guide 1.33. The licensee did not adequately control the modification of the ventilation

equipment used to vent airborne radioactive particulate to the refuel floor during reactor

vessel floodup. Consequently, while raising reactor vessel water level, the improper

venting led to personnel contaminations, uptakes of radioactive material, and the

3 Enclosure

evacuation of the Reactor Building. The licensee entered this issue into their corrective

action program and conducted an investigation into the event. The corrective actions

recommended the development and implementation of an acceptable methodology for

raising reactor water level.

This finding is more than minor because it affected the Occupational Radiation Safety

Cornerstone of Radiation Safety due to individual worker unplanned, unintended dose.

The finding was evaluated using the SDP and was determined to be a finding of very

low safety significance because there was not a substantial potential for overexposure

and the licensees ability to assess dose was not compromised. (Section 1R20)

B. Licensee-Identified Violations

A violation of very low safety significance, which was identified by the licensee, has been

reviewed by the inspectors. Corrective actions taken or planned by the licensee have

been entered into the licensees corrective action program. This violation and corrective

actions are listed in Section 4OA7 of this report.

4 Enclosure

REPORT DETAILS

Summary of Plant Status

Unit 2 began this inspection period shutdown for refueling outage 11 (RF11). Reactor

startup began on May 3 but was halted at 95 percent power on May 9 due to indications

of a fuel leak. Suppression testing commenced that same day, reducing reactor power

to approximately 63 percent until May 12 when the operators began increasing reactor

power after suppressing the fuel leak. On May 14, the reactor was at full power where it

remained at or near until May 19 when the operators began a reactor shutdown to

replace the leaking fuel assembly. After completing the work, operators began a reactor

startup on May 28. The reactor reached full power on May 30 where it remained at or

near until June 15 when an automatic reactor scram occurred as a result of a failure of

main unit transformer 2B. The failed transformer was disconnected and reactor startup

began on June 16. On June 21, the reactor reached 63 percent power (maximum

planned with transformer 2B out of service) and remained there for the remainder of the

inspection period.

1. REACTOR SAFETY

Cornerstone: Mitigating Systems, Barrier Integrity, Initiating Events, Emergency

Preparedness

1R01 Adverse Weather (71111.01A)

a. Inspection Scope

The inspectors reviewed licensee procedures for mitigating the effects of hot weather.

The inspectors reviewed severe weather procedures, emergency plan implementing

procedures related to severe weather, and annunciator response procedures, and

performed walkdowns. This included the reactor building and turbine building ventilation

preparations. Additionally, the inspectors reviewed condition assessment resolution

documents (CARD) and verified problems associated with adverse weather were

entered into the corrective action program with the appropriate significance

characterization.

These activities represented one hot weather systems preparation inspection sample.

b. Findings

No findings of significance were identified.

5 Enclosure

1R04 Equipment Alignments (71111.04)

.1 Partial System Walkdowns (71111.04Q)

a. Inspection Scope

The inspectors performed partial system walkdowns of the following risk-significant

systems:

C Safety Relief Valves performed the week of April 3, 2006;

C SLC A performed the week of April 24, 2006;

C Division II Residual Heal Removal (RHR) and Residual Heat Removal Service

Water (RHRSW) Lineup performed the week of May 14, 2006;

C Standby Electrical Power (emergency diesel generator [EDG]) lineup performed

the week of May 14, 2006; and

C Division I RHR and RHRSW Shutdown Cooling performed the week of

May 21, 2006.

The inspectors selected these systems based on their risk significance relative to the

reactor safety cornerstones. The inspectors reviewed operating procedures, system

diagrams, Technical Specification (TS) requirements, Administrative TS, and the impact

of ongoing work activities on redundant trains of equipment in order to identify

conditions that could have rendered the systems incapable of performing their intended

functions. The inspectors also walked down accessible portions of the systems to verify

system components were aligned correctly.

In addition, the inspectors verified equipment alignment problems were entered into the

corrective action program with the appropriate significance characterization.

These activities represented five quarterly partial system walkdown inspection samples.

b. Findings

No findings of significance were identified.

.2 Complete System Walkdown (71111.04S)

a. Inspection Scope

The inspectors performed a complete system walkdown of the following risk-significant

system:

The inspectors reviewed operating procedures, system diagrams, TS requirements, and

applicable sections of the Updated Final Safety Analysis Report (UFSAR) to ensure the

correct system lineup. The inspectors verified acceptable material condition of system

components, availability of electrical power to system components, and that ancillary

equipment or debris did not interfere with system performance.

6 Enclosure

These activities represented one semi-annual complete system walkdown inspection

sample.

b. Findings

No findings of significance were identified.

1R05 Fire Protection (71111.05)

.1 Routine Resident Inspector Tours (71111.05Q)

a. Inspection Scope

The inspectors conducted fire protection tours of the following risk-significant plant

areas:

  • Condensate Pump Room;
  • Standby Gas Treatment, Pipe Room;
  • Top of Torus;
  • RHR Complex, Division I EDG, Switchgear Rooms, Ventilation Rooms;
  • RHR Complex, Division I RHRSW Pump Room;
  • Division I, RHR Pump Room;
  • Division II, RHR Pump Room;
  • Main Unit Transformer 2B; and
  • Division II Electrical Switchgear Room.

The inspectors verified fire zone conditions were consistent with assumptions in the

licensee's fire hazards analysis. The inspectors walked down fire detection and

suppression equipment, assessed the material condition of fire fighting equipment, and

evaluated the control of transient combustible materials. In addition, the inspectors

verified fire protection related problems were entered into the corrective action program

with the appropriate significance characterization.

These activities represented eleven routine quarterly fire protection inspection samples.

b. Findings

No findings of significance were identified.

.2 RHR Complex, Division II EDG, Switchgear and Ventilation Rooms

a. Inspection Scope

The inspectors also conducted fire protection tours of the RHR complex, Division II

EDG, switchgear and ventilation rooms which are risk-significant plant areas.

7 Enclosure

The inspectors verified fire zone conditions were consistent with assumptions in the

licensee's fire hazards analysis. The inspectors walked down fire detection and

suppression equipment, assessed the material condition of fire fighting equipment, and

evaluated the control of transient combustible materials. In addition, the inspectors

verified fire protection related problems were entered into the corrective action program

with the appropriate significance characterization.

These activities represented one routine quarterly fire protection inspection sample.

b. Findings

Introduction: The inspectors identified an NCV of license condition 2.C(9) having very

low safety significance (Green) for the presence of unauthorized transient combustible

materials in the RHR complex.

Description: On May 15, 2006, the inspectors identified unauthorized transient

combustible materials in the RHR complex EDG 12 switchgear room. Specifically, the

inspectors identified an office chair and a plastic trash bin approximately half full of

paper secured approximately one foot from panel H21-P351, a safety-related electrical

panel for EDG 12 room ventilation, and associated cable raceway.

Section 9A.1.3.2.e of the UFSAR stated that the fire protection program had a

component to minimize the amount of combustibles to which safety-related areas may

be exposed. Procedure MOP11 implemented the fire protection program by prescribing

methods for controlling transient combustible material and the location of plant support

equipment. Step 3.5.1 of procedure MOP11 required a Plant Support Equipment

Approval form be obtained before placing any support equipment in the RHR complex.

The procedural requirement existed to ensure the introduction of transient combustible

materials was reviewed by fire protection personnel. However, no Plant Support

Equipment Approval form was submitted for the chair and trash bin identified in the

EDG 12 switchgear room within the RHR complex.

After the inspectors informed the fire protection supervisor of the issue, the fire

protection supervisor initiated CARD 06-23388 to initiate corrective actions. Licensee

personnel performed a walkdown of the RHR complex and identified three additional

trash bins and two chairs in other switchgear rooms within the RHR complex. The trash

bins and chairs were removed from the switchgear rooms.

Analysis: The inspectors determined the licensees failure to properly control transient

combustibles was a performance deficiency because the licensee is expected to comply

with their fire hazards analysis and because it was within the licensees ability to foresee

and prevent. The finding was greater than minor in accordance with Inspection Manual

Chapter (IMC) 0612, Power Reactor Inspection Reports, Appendix B, Issue

Disposition Screening, issued September 30, 2005, because the finding affected the

Mitigating Systems Cornerstone attribute for protection against external factors, i.e., fire.

Specifically, a fire involving the unauthorized transient combustibles could have affected

a nearby electrical panel and associated cable raceway containing mitigating system

equipment important to safety. The inspectors identified that a credible fire scenario

existed in that equipment important to safety was located within the zone of influence of

8 Enclosure

the unauthorized transient combustible materials as described by Table 2.3.2,

Calculated Values (in feet) for Use in the Ball and Column Zone of Influence Chart for

Fires in an Open Location Away from Walls of IMC 0609, Appendix F, Fire Protection

Significance Determination Process, issued February 28, 2005.

The inspectors completed a significance determination of this issue using IMC 0609,

Appendix F. The inspectors reviewed IMC 0609, Appendix F, Attachment 2,

Degradation Rating Guidance Specific to Various Fire Protection Program Elements,

and determined the unauthorized transient combustible materials represented a low

degradation rating because the materials would not have ignited from existing sources

of heat or electrical energy. As such, the finding screened to Green under Question 1 of

IMC 0609, Appendix F, Task 1.3.1, Qualitative Screening for All Finding Categories,

and was considered a finding of very low safety significance. The primary cause of this

finding was related to the cross-cutting aspect of problem identification and resolution

because the licensees response to several recent instances of unauthorized transient

combustibles was not effective in preventing this instance of unauthorized transient

combustibles.

Enforcement: License condition 2.C.(9) required the licensee to implement and

maintain in effect all provisions of the approved fire protection program as described in

the UFSAR. Section 9A.1.3.2.e of the UFSAR stated the fire protection program had a

component to minimize the amount of combustibles to which safety-related areas may

be exposed. Procedure MOP11 implemented the fire protection program by prescribing

methods for controlling transient combustible material and the location of plant support

equipment. Step 3.5.1 of procedure MOP11 required a Plant Support Equipment

Approval form be obtained before placing any support equipment in the RHR complex, a

safety-related area. Contrary to the above, on May 15, 2006, the inspectors identified

support equipment, i.e., a chair and a trash bin, had been placed in the EDG 12

switchgear room within the RHR complex without a Plant Support Equipment Approval

form having been obtained. Once identified, the licensee initiated CARD 06-23388,

performed a walkdown of the RHR complex, and removed unauthorized chairs and trash

bins from the switchgear rooms in the RHR complex. Because this violation is of very

low safety significance and because it was entered into the licensees corrective action

program as CARD 06-23388, this violation is being treated as an NCV, consistent with

Section VI.A.1 of the NRC Enforcement Policy: NCV 05000341/2006003-01:

Unauthorized Transient Combustibles in Safety-Related Areas.

.3 Fire Protection - Drill Observation (71111.05A)

a. Inspection Scope

The inspectors assessed fire brigade performance and the drill evaluators' critique

during an unannounced fire brigade drill on June 21, 2006. The drill simulated a fire in

the chemical storage room in the radioactive waste building. The inspectors focused on

the command and control of fire brigade activities, fire fighting and communication

practices, material condition and use of fire fighting equipment, and implementation and

adequacy of pre-planned fire fighting strategies.

9 Enclosure

These activities represented one annual fire protection - drill observation inspection

sample.

b. Findings

Introduction: The inspectors identified a Green NCV of license condition 2.C(9) for the

failure to appropriately store chemicals in accordance with the fire hazards analysis.

Description: The inspectors watched Fire Brigade Drill Scenario Number 6 which

involved a simulated fire in the chemical storage room on the first floor of the radioactive

waste building. Firefighters entered the room wearing full protective clothing and

positive-pressure, self-contained breathing apparatus. In accordance with fire protection

Pre-Plan FP-RDWST, Rev. 4, Radioactive Waste Building Zones 22, 23, 24, and 25, the

brigade simulated extinguishing the fire by using a water hose in a fog pattern.

The inspectors later questioned the adequacy of the fire protection pre-plan because it

did not appear to take into account differences in fire fighting strategies with the various

types of chemicals in the room. After reviewing the list of chemicals in the room against

the fire fighting strategies recommended by NFPA-49, Hazardous Chemicals Data 1994

Edition, the inspectors identified four chemicals normally stored in the room where

NFPA-49 recommends using special protective clothing when fighting a fire involving

those chemicals: monoethylamine solution, sodium hydroxide, potassium hydroxide,

and sulfuric acid. Additionally, NFPA-49 recommends against the use of water when

fighting fires involving sulfuric acid.

The inspectors reviewed the storage locations of these chemicals and determined they

were not segregated in such a manner to ensure a fire in that room did not involve any

of those chemicals. Further, the fire protection pre-plan contained no guidance on any

special precautions to be followed when fighting a fire involving any of those four

chemicals. The inspectors determined it was unreasonable to assume the responding

fire brigade would be able to easily determine what chemicals were on fire given the lack

of labeling and amount of smoke that likely would be present in the room during an

actual fire.

The licensees fire hazards analysis, as documented in UFSAR, Section 9A.5.G.3,

required chemicals be stored in accordance with the guidelines of NFPA-49. Although

the literal storage requirements for these chemicals were generally adhered to, e.g.,

stored in a cool, dry, ventilated room in metal cabinets, etc., the inspectors determined

the fire fighting strategies for the four chemicals of interest above were inseparable from

the storage guidelines because the licensee is expected to take all relevant information

into account when determining the appropriate chemical storage requirements. For

example, although NFPA-49 contained no guidance to store sulfuric acid separately

from nitric acid, the fact that water is suitable for fires involving nitric acid but not for fires

involving sulfuric acid logically concludes either, a) water should not be used if the

chemicals are in the same cabinet, b) the sulfuric acid should be stored in a separate

container, or c) the quantity of sulfuric acid is controlled sufficiently low so as to not

require segregation; none of which occurred. Likewise, because chemical suits are

recommended for those four chemicals but standard fire fighter turnout gear is suitable

for all other normally stored chemicals in the room, it is reasonable to expect the

10 Enclosure

licensee will take the emergency response personal protective equipment guidelines into

account when storing chemicals which the licensee also failed to do.

The inspectors questioned the licensee on how chemicals were controlled such that they

did not adversely affect the fire protection strategy and were informed that chemicals

are evaluated based on the effect they would have on the plant but not on the effect

they would have on fire fighting techniques. For example, there were no controls in

place to either ensure the fire brigade did not use water on fires involving sulfuric acid or

to control the amount of sulfuric acid below some threshold to preclude any alteration in

the fire fighting strategy.

Analysis: The inspectors determined the licensees failure to properly store chemicals in

accordance with guidelines contained in NFPA 49 was a performance deficiency

because the licensee is expected to comply with their fire hazards analysis and because

it was within the licensees ability to foresee and prevent. The finding is more than

minor because it represented a programmatic deficiency in the licensees chemical

control program which affected the ability of the fire brigade to respond to and mitigate

the effects of a fire. This finding affected the emergency planning cornerstone because

it affected the ability of the fire brigade to respond to a fire which could potentially affect

the licensees emergency plan.

The finding is not suitable for SDP evaluation, but has been reviewed by NRC

management and is determined to be a finding of very low safety significance (Green)

because the quantities of the relevant chemicals were low and the storage location was

sufficiently remote from mitigating equipment.

Enforcement: Fermi 2 Facility Operating License NPF-43, condition 2.C(9), required,

in part, that the licensee implement and maintain in effect all provisions of the

approved fire protection program as described in Section 9A of the UFSAR as

amended and approved in the Fermi 2 safety evaluation report through supplement 6.

UFSAR 9A.5.G.3 required hazardous chemicals be stored in accordance with the

guidelines of NFPA 49-1994, Hazardous Chemicals Data 1994 Edition. Contrary to

the above, on June 21, 2006, the licensee failed to utilize the guidelines contained in

NFPA 49-1994 when storing chemicals in the radioactive waste building. Because

this violation is of very low safety significance and because it was entered into the

licensees corrective action program as CARD 06-24243, this violation is being

treated as an NCV, consistent with Section VI.A.1 of the NRC Enforcement Policy:

NCV 05000341/2006003-02: Improper Storage of Chemicals Affecting Fire Fighting

Response.

1R06 Flood Protection (71111.06)

a. Inspection Scope

The inspectors performed an inspection related to the licensee's precautions to mitigate

the risk from internal flooding events. The inspectors performed a walkdown of the

following plant areas to assess the adequacy of watertight doors and verify drains and

sumps were clear of debris and were operable:

11 Enclosure

  • Auxiliary Building T Room.

The inspectors also reviewed the work activities associated with internal flooding to

verify identified problems were being entered into the corrective action program with the

appropriate characterization and significance.

These activities represented one internal flood protection inspection sample.

b. Findings

No findings of significance were identified.

1R07 Heat Sink Performance (71111.07A)

a. Inspection Scope

The inspectors reviewed completed test reports and observed the performance of

inspections for the RHR service water heat exchanger.

The inspectors selected this heat exchanger because its associated systems were risk

significant in the licensee's risk assessment and were required to support the operability

of other risk-significant, safety-related equipment. During these inspections, the

inspectors observed the as-found condition of the heat exchanger and verified no

deficiencies existed that would mask degraded performance. The inspectors discussed

the as-found condition as well as the historical performance of the heat exchanger with

engineering department personnel and reviewed applicable documents and procedures.

In addition, the inspectors verified heat sink problems were entered into the corrective

action program with the appropriate significance characterization, and completed

corrective actions were adequate and appropriately implemented.

These activities represented one heat sink performance inspection sample.

b. Findings

No findings of significance were identified.

1R11 Licensed Operator Requalification (71111.11Q)

a. Inspection Scope

On June 13, 2006, the inspectors observed an operations support crew during the

annual requalification examination in mitigating the consequences of events in

SS-OP-802-330, Anticipated Transient Without Scram with Small Steam Leak, Rev. 0,

dated January 26, 2006, on the simulator. The inspectors evaluated the following areas:

12 Enclosure

C licensed operator performance;

C crews clarity and formality of communications;

  • ability to take timely actions in the conservative direction;
  • prioritization, interpretation, and verification of annunciator alarms;
  • correct use and implementation of abnormal and emergency procedures;

C control board manipulations;

C oversight and direction from supervisors; and

C ability to identify and implement appropriate TS actions and Emergency Plan

actions and notifications.

The crews performance in these areas was compared to pre-established operator

action expectations and successful critical task completion requirements.

These activities represented one quarterly licensed operator requalification inspection

sample.

b. Findings

No findings of significance were identified.

1R12 Maintenance Effectiveness (71111.12Q)

a. Inspection Scope

The inspectors evaluated degraded performance issues involving the following three

risk-significant systems:

C Station Blackout Diesel Generators CTG 11-1, 2, 3, 4, and 120 kV switchyard;

C RHR System A and B; and

C Molded Case Circuit Breakers.

The inspectors assessed performance issues with respect to the reliability, availability,

and condition monitoring of the system. Specifically, the inspectors independently

verified the licensee's actions to address system performance or condition problems in

terms of the following:

C implementing appropriate work practices;

C identifying and addressing common cause failures;

C scoping of systems in accordance with 10 CFR 50.65(b);

C characterizing system reliability issues;

C tracking system unavailability;

C trending key parameters (condition monitoring);

C ensuring 10 CFR 50.65(a)(1) or (a)(2) classification and/or re-classification; and

C verifying appropriate performance criteria for systems classified as (a)(2) and/or

appropriate and adequate goals and corrective actions for systems classified as

(a)(1).

In addition, the inspectors verified maintenance effectiveness issues were entered into

the corrective action program with the appropriate significance characterization.

13 Enclosure

These activities represented three quarterly maintenance effectiveness inspection

samples.

b. Findings

No findings of significance were identified.

1R13 Maintenance Risk Assessments and Emergent Work Control (71111.13Q)

.1 Routine Maintenance Risk Assessments

a. Inspection Scope

The inspectors reviewed the licensee's evaluation and management of plant risk for the

maintenance and operational activities affecting risk-significant and safety-related

equipment listed below:

  • maintenance risk for week of April 2, 2006;
  • maintenance risk for week of April 17, 2006;
  • maintenance risk for week of April 30, 2006; and
  • maintenance risk for week of June 26, 2006.

These activities were selected based on their potential risk significance relative to the

reactor safety cornerstones. As applicable for each activity, the inspectors reviewed the

scope of maintenance work, discussed the results of the assessment with the licensee's

probabilistic risk analyst and/or shift technical advisor, and verified plant conditions were

consistent with the risk assessment. The inspectors also reviewed TS requirements and

walked down portions of redundant safety systems, when applicable, to verify risk

analysis assumptions were valid and applicable requirements were met.

These activities represented four quarterly maintenance risk assessment and

emergency work control inspection samples.

b. Findings

No findings of significance were identified.

.2 Inadequate Maintenance Risk Assessment

a. Inspection Scope

The inspectors reviewed the activities surrounding the Division I battery load test

performed during RF11 to determine if the licensee appropriately considered the risk

impacts of performing the test. The inspectors interviewed licensee staff, reviewed

documents, and performed walkdowns. The inspectors considered ancillary equipment

affected by the test to determine what affect, if any, the test would have on it.

These activities represented one quarterly maintenance risk assessment and

emergency work control inspection sample.

14 Enclosure

b. Findings

Introduction: The inspectors identified a Green NCV of 10 CFR 50.65(a)(4) for the

failure to perform an adequate risk assessment for the Division I battery load test.

Description: On April 3, 2006, the inspectors identified a temporary fan installed in the

blocked-open doorway to the dc motor control center (DC MCC) area. Upon entering

the room, the inspectors noticed that additional doors inside the DC MCC area leading

to each of the reactor protection system motor generator (RPSMG) set rooms were

open. After questioning why the doors were blocked open and a fan installed, the

inspectors learned operators took those actions to provide additional cooling to the

RPS MG sets because the Division I 130/260 VDC battery load surveillance test,

procedure 42.309.05, was in progress.

Because the air-cooled load bank used for the test was temporarily installed in the

DC MCC area, temperatures in the room started to increase after the test commenced.

However, two area room coolers were out of service due to a scheduled outage of the

GSW system which left the DC MCC, vital battery, battery charger, and RPS MG set

rooms with no cooling. In order to help prevent a loss of shutdown cooling, which would

have occurred had the RPS MG sets tripped, the operators had previously blocked

opened the doors to the RPS MG set rooms which further increased the temperature in

the DC MCC area. Operators then blocked open the double doors to the DC MCC area

and installed a large utility fan in the doorway to provide additional cooling to the area.

The test was successfully completed, temperatures dropped, and the fan was removed.

The outage risk associated with this test did not consider the effects it would have on

the key safety function of maintaining decay heat available due to the additional heat

from the load bank with no room cooling. Moreover, the outage risk associated with the

GSW outage assumed that the RPS MG sets would not be running. Consequently,

prudent risk management actions were not developed prior to performing the battery

load test. However, because operators installed a fan in the open doorway early

enough into the test, shutdown cooling remained in operation.

Analysis: The inspectors determined the failure to perform an adequate risk analysis of

maintenance activities prior to performing maintenance was a performance deficiency

because the licensee is expected to comply with the requirements of the maintenance

rule. This finding is more than minor because the licensees risk assessment failed to

consider maintenance activities that could increase the likelihood of an initiating event,

specifically a loss of shutdown cooling. In addition, this finding affected the initiating

event cornerstone because it is associated with an increase in the likelihood of an

initiating event. The inspectors utilized the maintenance risk and shutdown risk SDP to

assess the risk of this finding. The finding is of very low safety significance because the

finding did not affect the ability of operators to recover from a loss of shutdown cooling

had it occurred. The inspectors determined the cause of this finding impacted the

Human Performance cross-cutting area because the cause of the inadequate risk

assessment was due to a personnel error.

Enforcement: 10 CFR 50.65(a)(4) requires, in part, that before performing

maintenance activities, the licensee shall assess and manage the increase in risk

15 Enclosure

that may result from the proposed maintenance activities. Contrary to the above,

beginning on April 1, 2006, and continuing through April 6, 2006, the licensee

performed surveillance procedure 42.309.05 without adequately assessing and

managing the increase in risk prior to performing the activity. Because this violation is

of very low safety significance and because it was entered into the licensees corrective

action program as CARD 06-21892 and 06-24495, this violation is being treated as an

NCV, consistent with Section VI.A.1 of the NRC Enforcement Policy:

NCV 05000341/2006003-03: Inadequate Maintenance Risk Assessment.

1R14 Personnel Performance During Non-Routine Plant Evolutions and Events (71111.14)

a. Inspection Scope

The inspectors reviewed the licensees actions in response to the following non-routine

events to ensure the licensee took appropriate actions in accordance with licensee

procedures:

  • unplanned reactor building contamination, CARD 06-21534;
  • control rod position indication malfunction, CARD 06-23491 & 06-23489;
  • mode 5 reactor scram during installation of shorting links, CARD 06-23588.

The inspectors reviewed operator logs, procedures, corrective action documents, other

documents, and interviewed personnel. The inspectors also evaluated the licensees

operational decision making involved with these non-routine events.

These activities represented four inspection samples.

b. Findings

No findings of significance were identified.

1R15 Operability Evaluations (71111.15)

.1 Routine Review of Operability Evaluations

a. Inspection Scope

The inspectors reviewed the following documents to ensure the identified condition did

not render the involved equipment inoperable or result in an unrecognized increase in

plant risk, and the licensee appropriately applied TS limitations and appropriately

returned the affected equipment to an operable status:

  • CARD 06-23114, Motor Operator Valve Motor Replacement for RHR Shutdown

Cooling Inboard Suction Bypass Valve; and

Pump In-Service Test Flow Unattainable.

These activities represented two operability evaluation inspection samples.

16 Enclosure

b. Findings

No findings of significance were identified.

.2 Standby Liquid Control Operability During Air Sparging Operations

a. Inspection Scope

The inspectors reviewed the licensees practice of placing an air sparge on the SLC tank

to determine if system operability was justified. The inspectors reviewed previous

engineering evaluations to determine the technical adequacy of the conclusions. The

inspectors reviewed operator logs, TS, design basis documents, UFSAR, and other

documents. The inspectors interviewed operators, engineers, and other licensee staff.

These activities represented one operability evaluation inspection sample.

b. Findings

Introduction: The inspectors identified a Green NCV of TS for the SLC system being

inoperable for longer than the action time to be in hot shutdown with both SLC

subsystems inoperable.

Description: In April 1999, the licensee reviewed an operating experience report issued

by another licensee discussing the inoperability of the SLC system during air sparging

activities. Air sparging the SLC tank was done to facilitate mixing of the sodium

pentaborate in the tank and was performed prior to the monthly chemistry analysis and

after any chemical addition to the tank. The air sparge header was located near the

bottom of the tank in proximity to the SLC pump suction line. The concern was that if

the pumps were operating while the air sparge was operating, air could be drawn into

the pumps and compromise their ability to perform their design function. The licensee

initiated CARD 99-13240 to evaluate the applicability of the issue to Fermi.

The licensee determined that although pump performance would be impacted if the

pumps were required while an SLC tank air sparge was in progress, the pumps

remained operable. Based on input from the pump vendor, the licensee concluded that

entrained air in the pumped water would cause increased pump vibration and a

negligible reduction in delivered flow rate. Because the vendor stated the increased

vibration would only affect long-term pump reliability, the licensee concluded that

long-term pump degradation was not a concern because SLC had a 2 hour2.314815e-5 days <br />5.555556e-4 hours <br />3.306878e-6 weeks <br />7.61e-7 months <br /> mission

time.

In an effort to lessen the probability of requiring the SLC pumps during an actual event

while the air sparge was operating, the licensee identified the need to revise the system

operating procedures to minimize duration of sparge operations from hours to minutes.

The action to revise procedure 23.149, Standby Liquid Control System, was originally

due on June 30, 1999.

The inspectors reviewed the licensees evaluation and noted the CARD did not contain

either any documentation from the vendor or any attempt to quantify the reduction in

17 Enclosure

flow rate to ensure the minimum required flow was maintained. The inspectors asked

the licensee for the vendors recommendations in writing but were later told the pump

vendor declined to support their previous conclusion in writing. The inspectors were

concerned that if the pump vendor was unwilling to state in writing that the pumps would

operate for at least 2 hours2.314815e-5 days <br />5.555556e-4 hours <br />3.306878e-6 weeks <br />7.61e-7 months <br /> during sparging, then pump operability was not justified.

The inspectors brought their concern to the licensee who entered the issue into their

corrective action program as CARD 06-23785 on June 1, 2006. After further review, the

licensee concluded that SLC operability during sparging could not be supported and

revised procedure 23.149 accordingly. Upon review of control room logs, the inspectors

determined that although the licensee significantly reduced the total sparging time since

1999, the tank was air sparged for 21 hours2.430556e-4 days <br />0.00583 hours <br />3.472222e-5 weeks <br />7.9905e-6 months <br /> on August 24, 1999, which exceeded the

time to be in hot shutdown of 20 hours2.314815e-4 days <br />0.00556 hours <br />3.306878e-5 weeks <br />7.61e-6 months <br /> with both SLC subsystems inoperable while in

Mode 1 or 2. In addition, the inspectors concluded the maximum unavailability in any

1-year period after identification of the issue in 1999 was approximately 90 hours0.00104 days <br />0.025 hours <br />1.488095e-4 weeks <br />3.4245e-5 months <br />.

Analysis: The inspectors determined the licensees failure to appropriately evaluate

SLC operability during sparging operations was a performance deficiency because the

licensee is expected to adequately evaluate issues that affect the operability of TS

equipment and because it was within the licensees ability to foresee and prevent. The

finding is more than minor because it affected the equipment performance attribute of

the reactor safety cornerstone objective of ensuring the availability, reliability, and

capability of mitigating equipment to respond to initiating events to prevent undesirable

consequences.

The inspectors assessed the finding using the SDP. Because the inspectors

considered this finding to represent an actual loss of a safety function of SLC, the

inspectors performed a phase 2 SDP analysis. A phase 3 analysis was subsequently

performed by the senior reactor analyst (SRA). The SRA performed the risk evaluation

using the Fermi Standardized Plant Analysis Risk (SPAR) Model, Level 1, Revision 3P,

Change 3.21, created October 2005. The SRA ran the SPAR model assuming common

cause failure of both SLC pumps, with an exposure time of 90 hours0.00104 days <br />0.025 hours <br />1.488095e-4 weeks <br />3.4245e-5 months <br />. Using the above

information the SRA obtained a change in core damage frequency (CDF) of 3.1E-8

(Green) for internal events. The dominant sequences involved a failure of the reactor to

scram after a transient, loss of condenser heat sink, and loss of main feedwater, and

failure of the SLC system.

Anticipated transient without scram events are not assumed to be caused by external

events and, therefore, the risk contribution from external events is insignificant.

Similarly, because the internal events CDF is less than 1E-7, large early release

frequency (LERF) is not significant per IMC 0609, Appendix H. The SRA concluded

the total CDF considering internal events, external events, and LERF is estimated at

3.1E-8 (Green).

Enforcement: Technical Specification 3.1.5.a.2, Amendment 38, required that while in

Modes 1 and 2, with the SLC system otherwise inoperable, the licensee must restore

the system to operable status within 8 hours9.259259e-5 days <br />0.00222 hours <br />1.322751e-5 weeks <br />3.044e-6 months <br /> or be in at least hot shutdown within the

next 12 hours1.388889e-4 days <br />0.00333 hours <br />1.984127e-5 weeks <br />4.566e-6 months <br /> and was in effect on August 24 and 25, 1999. Contrary to the above,

beginning on August 24, 1999, and continuing until August 25, 1999, while in Modes 1

18 Enclosure

and 2, the SLC system was inoperable for 21 hours2.430556e-4 days <br />0.00583 hours <br />3.472222e-5 weeks <br />7.9905e-6 months <br /> while the SLC tank was being air

sparged; therefore, on August 25, 1999, with the SLC system inoperable for greater

than 20 hours2.314815e-4 days <br />0.00556 hours <br />3.306878e-5 weeks <br />7.61e-6 months <br />, the plant was not in at least hot shutdown. Because this violation is of

very low safety significance and because it was entered into the licensees corrective

action program as CARD 06-23785, this finding is being treated as an NCV, consistent

with Section VI.A.1 of the NRC Enforcement Policy: NCV 05000341/2006003-04:

Improper Evaluation of Standby Liquid Control Operability During Tank Sparging.

.3 Inappropriate Use of Risk in Operability Evaluations

a. Inspection Scope

The inspectors reviewed CARD 06-23913 to ensure that the identified condition did not

render the involved equipment inoperable or result in an unrecognized increase in plant

risk and that the licensee appropriately applied TS limitations and appropriately returned

the affected equipment to an operable status.

These activities represented one operability evaluation inspection sample.

Introduction: The inspectors identified an Unresolved Item (URI) when the licensee

removed pipe insulation, credited for environmental qualification of nearby equipment,

while at power without an adequate engineering evaluation.

Description: On June 8, 2006, the licensee initiated CARD 06-23913 to request a work

request to replace contaminated insulation on the suction and discharge pipe for the B

RHR pump. As a result, Work Request (WR) 000Z062027 was released and work

began on June 13, 2006. While performing a plant tour on June 15, 2006, the

inspectors identified the insulation was missing from the suction pipe for the B RHR

pump and questioned the licensee if the insulation removal had an approved

engineering evaluation. Because the equipment was in a potentially harsh environment,

the uninsulated pipe would increase the temperature profile of the room during accident

conditions which could affect the environmental qualification of electrical equipment in

the room. The licensee stated the evaluation was documented in CARD 06-23913 and

concluded that removing the insulation while at power was acceptable.

The inspectors reviewed the subject evaluation and became concerned that one of the

assumptions for the evaluation was that an accident was not considered as credible

during the period of time the insulation was to be removed. Upon further review, the

inspectors learned the licensee used non-accident heat loads to determine the

environmental effects of removing the insulation. The licensees justification was that if

the total time the insulation was removed was less than 168 hours0.00194 days <br />0.0467 hours <br />2.777778e-4 weeks <br />6.3924e-5 months <br />, then the probability

of either a high energy line break or loss of coolant accident was negligible and, hence,

did not need to be assumed to occur.

The definition of operability stated, however, the equipment must be capable of

performing its specified function(s). The inherent assumption was the occurrence,

conditions, or event would exist and the safety function could be performed. Therefore,

19 Enclosure

the inspectors concluded the use of probabilities of the occurrence of accidents while

the insulation was removed was an unacceptable assumption in the subsequent

operability evaluation.

While reviewing this evaluation, the inspectors discovered the licensee used the

same method of evaluating on-line insulation removal since at least September 20,

2001, and found five additional CARDs where the licensee approved removing

insulation from equipment in potentially harsh areas while at power, likewise with

unacceptable evaluations. Because the extent of condition of this issue is potentially

significant and could extend to work other than on-line insulation removal, this item is

unresolved pending the inspectors review of the licensees full extent of condition

review and subsequent risk evaluation and is identified as Unresolved Item

(URI) 05000341/2006003-05: Inappropriate Use of Risk in Operability Evaluations.

1R19 Post-Maintenance Testing (71111.19)

a. Inspection Scope

The inspectors reviewed post-maintenance testing (PMT) activities associated with the

following scheduled maintenance:

  • Drywell Cooler Number 4 Replacement, WR 000Z052131;

WR 000Z050487;

  • WR 000Z060156, Replace Control Rod Drive Pump Inboard Bearing Oil Level

Sight glass.

The inspectors reviewed the scope of the work performed and evaluated the adequacy

of the specified PMT. The inspectors verified the PMT was performed in accordance

with approved procedures, the procedures clearly stated acceptance criteria, and the

acceptance criteria were met. The inspectors interviewed operations, maintenance, and

engineering department personnel and reviewed the completed PMT documentation.

In addition, the inspectors verified PMT problems were entered into the corrective action

program with the appropriate significance characterization.

These activities represented seven PMT inspection samples.

b. Findings

No findings of significance were identified.

20 Enclosure

1R20 Refueling and Outage Activities (71111.20)

.1 Routine Refueling Outage Inspection Activities

a. Inspection Scope

The inspectors observed the licensees performance during RF11, which was in

progress at the beginning of this inspection and concluded on May 5, 2006.

This inspection consisted of a review of the licensees outage schedule, safe shutdown

plan and administrative procedures governing the outage, periodic observations of

equipment alignment, and plant and control room outage activities. Specifically, the

inspectors determined whether the licensee effectively managed elements of shutdown

risk pertaining to reactivity control, decay heat removal, inventory control, electrical

power control, and containment integrity.

The inspectors performed the following activities daily, during the outage:

  • attended control room operator and outage management turnover meetings to

verify the current shutdown risk status was well understood and communicated;

  • performed walkdowns of the main control room to observe the alignment of

systems important to shutdown risk;

compared channels and trains against one another;

  • performed walkdowns of the turbine, auxiliary, and reactor buildings and the

drywell to observe ongoing work activities, to ensure work activities were

performed in accordance with plant procedures, and to verify procedural

requirements regarding fire protection, foreign material exclusion, and the

storage of equipment near safety-related structures, systems, and components

were maintained;

requirements; and

  • reviewed selected issues the licensee entered into its corrective action program

to verify identified problems were being entered into the program with the

appropriate characterization and significance.

Additionally, the inspectors performed the following specific activities:

  • monitored refueling activities to verify the licensee adhered to established

procedures and TS requirements for handling of irradiated fuel;

  • performed drywell closeout;
  • verified completion of restart restraint items; and
  • observed control rod withdrawal to criticality and portions of the plant power

ascension.

In particular, the inspectors reviewed the licensees restart restraint process and verified

the closure of selected issues. Documents reviewed during these inspection activities

are listed at the end of this report.

21 Enclosure

Because inspection activities for this refueling outage constituted one inspection sample

in Inspection Report 05000341/2006002, and since only one sample is counted per

outage, the inspection activities for this inspection period do not constitute an additional

refueling and outage inspection sample.

b. Findings

Introduction: The inspectors identified a Green NCV of Technical Specification 5.4.1.a,

for the failure to adequately control the modification of the ventilation equipment used to

vent airborne radioactive particulate to the refuel floor during reactor vessel floodup.

Description: At 1450, on March 26, 2006, operators initiated core spray at approximately

3000 gpm to raise reactor water level, to permit removal of the reactor vessel head. The

reactor vessel head vent pipe had been disconnected, to permit installation of a

ventilation unit for the venting of gases to the refuel floor. The ventilation unit consisted

of a nominal 3600 scfm fan, a charcoal filter, and a HEPA particulate filter. Neither filter

had been recently tested. The ventilation unit was configured with two hoses placed to

take suction close to the reactor vessel head vent. The exhaust of the ventilation unit

ran to a point below an intake for the Standby Gas Treatment System (SGTS), to permit

capture of the exhaust by the SGTS.

At approximately 1500, the ventilation unit intake hoses were observed being pushed

away from the reactor vessel head vent, due to flow from the vent. Core spray was shut

down at 1502 and at 1504 visible moisture was seen being emitted from the vent. A

continuous air monitor on the refuel floor alarmed at 1510 and RP ordered the

evacuation of all but essential personnel from the refuel floor. By 1525 all personnel

were removed from the floor and shortly after this, the entire reactor building was

evacuated due to the spread of contamination. Decontamination of several workers was

required. Twenty-eight workers were whole body counted, with 26 showing uptakes of

varying levels of Co-60, Co-58, and Mn-54.

There were three conditions that contributed to the cause of the event. First of all,

coolant activity levels were higher than expected due to a crud burst during shutdown

and the temporary loss of RWCS allowed Co-60 to enter and remain in the coolant,

possibly plating out on reactor internals. The second condition related to the

temperature of the material vented from the reactor vessel head. Reactor vessel

outside shell temperatures indicated 215 degrees F, which equates to internal metal

temperatures above the atmospheric boiling point of water. This indicates that some of

the coolant flashed to steam as the level in the reactor vessel rose, which could increase

the carryover of coolant activity to the vented gas. The third condition was the

inadequate processing of vented material from the reactor vessel head. The venting of

the airborne radioactive particulate would not have resulted in building contamination

and personnel uptakes if the ventilation unit had effectively removed this material to the

SGTS.

The use of the ventilation system was not in accordance with its design configuration.

The ventilation system for previous outages had suction hoses connected to a hood that

was placed over the reactor vessel head vent, to improve the capture of vented material.

The use of the hood was discontinued due to its impact on water level instrumentation.

22 Enclosure

An engineering evaluation was not performed on the impact of the change in

configuration of the ventilation system. In addition, the exhaust arrangement from the

ventilation unit to the SGTS had not been evaluated for effectiveness. Licensee

Procedure MES12, Performing Temporary Modifications, requires the modification

process be followed and an evaluation be performed.

Furthermore, licensee procedural guidance did not exist for the overall process of taking

the operating reactor to a condition allowing fuel movement. The event could have been

prevented if appropriate acceptance criteria for allowable reactor vessel temperature

and coolant activity levels existed. Thus, the root cause of the event was determined to

be a procedural and programmatic weakness.

The licensee initiated CARD 06-21534, Continuous Air Monitor Alarm on Refueling

Floor, to track the investigation of the event in their CAP. The primary corrective action

recommendation is to develop and implement an acceptable methodology for raising

reactor vessel water level. In addition, the design and configuration of the current

ventilation exhaust capture system will be evaluated and modified, as appropriate to

assure that it is adequate for the expected reactor vessel fill rate and radioactive

material concentrations. The methodology may involve an alternate vent path, such as

using the attached piping to vent the reactor vessel to the drywell.

Analysis: The inspectors determined the licensees lack of control of the Temporary

Modification process constituted a design control issue. The licensees failure to

adequately control the process used to vent airborne radioactive particulate to the refuel

floor during reactor vessel floodup represents a performance deficiency as defined in

NRC Inspection Manual Chapter 0612, Appendix B, Issue Screening. The issue was

determined to be more than minor because if left uncorrected the issue could become a

more significant safety concern if coolant activity levels were higher or if the vessel was

flooded quicker.

The finding was assessed using NRC Inspection Manual Chapter 0609, Appendix C,

Occupational Radiation Safety Significance Determination Process due to individual

worker unplanned, unintended dose. The finding was determined to be of very low

safety significance because the inspectors answered, NO, to all four phase 1

screening questions.

Enforcement: Technical Specification 5.4.1.a requires that procedures recommended in

Regulatory Guide 1.33, Revision 2, Appendix A, February 1978, be established,

implemented and maintained. Section 4.a of that document, in part requires

instructions for filling, venting, and draining the reactor pressure vessel. Contrary to the

above, the initial installation of the ventilation system and the changes made to the

ventilation system that was used as part of the reactor vessel floodup during outages

was not processed through the Temporary Modification Procedure. This finding is being

treated as an NCV, consistent with Section VI.A.1 of the NRC Enforcement Policy and is

identified as NCV 05000341/2006003-06: Inadequate Controls for Venting the Reactor

Pressure Vessel Head. This issue is in the licensees corrective action program as

CARD 06-22667.

23 Enclosure

.2 Forced Outage 06-01

a. Inspection Scope

The inspectors observed the licensees performance during Forced Outage 06-01 from

May 20, 2006, through May 29, 2006, which was scheduled to locate and replace a

failed fuel assembly. During power ascension following RF11, operators identified a

potential fuel leak because off gas radiation levels were slightly elevated from normal.

Operators began suppression testing later that day, which identified the failed assembly.

Operators initiated a manual unit shutdown to replace the failed fuel. While the unit was

shutdown, additional assemblies subjected to similar flux profile histories were also

replaced although fuel sipping operations identified only one fuel assembly with a fuel

cladding defect.

This inspection consisted of a review of the licensees outage schedule, safe shutdown

plan and administrative procedures governing the outage, periodic observations of

equipment alignment, and plant and control room outage activities. Specifically, the

inspectors determined whether the licensee effectively managed elements of shutdown

risk pertaining to reactivity control, decay heat removal, inventory control, electrical

power control, and containment integrity.

The inspectors performed the same daily activities, during the outage as described in

Section 1R20.1 for the refueling outage.

These activities represented one forced outage inspection sample.

b. Findings

No findings of significance were identified.

.3 Forced Outage 06-02

a. Inspection Scope

The inspectors observed the licensees performance during Forced Outage 06-02 from

June 15, 2006, through June 17, 2006. On June 15, a reactor scram occurred due to a

main turbine generator trip which occurred when main unit transformer 2B failed. The

inspectors responded to the control room and to the transformer area to assess the

licensees response to the event.

This inspection consisted of a review of the licensees outage schedule, safe shutdown

plan and administrative procedures governing the outage, and plant and control room

outage activities. Specifically, the inspectors determined whether the licensee

effectively managed elements of shutdown risk pertaining to reactivity control, decay

heat removal, inventory control, and electrical power control.

24 Enclosure

The inspectors performed the following activities during the outage:

  • attended control room operator and outage management turnover meetings to

verify the current shutdown risk status was well understood and communicated;

  • performed walkdowns of the main control room to observe the alignment of

systems important to shutdown risk;

  • observed the operability of RCS instrumentation and compared channels and

trains against one another; and

  • observed control rod withdrawal to criticality and portions of the plant power

ascension.

These activities represented one forced outage inspection sample.

b. Findings

No findings of significance were identified.

1R22 Surveillance Testing (71111.22Q)

a. Inspection Scope

The inspectors reviewed the test results for the following activities to determine whether

risk-significant systems and equipment were capable of performing their intended safety

function and to verify testing was conducted in accordance with applicable procedural

and TS requirements:

  • MSIV Channel Functional Test (isolation valve);
  • LOOP/LOCA Test (routine);

(routine); and

Pressure (routine).

The inspectors reviewed the test methodology and test results to verify equipment

performance was consistent with safety analysis and design basis assumptions. In

addition, the inspectors verified surveillance testing problems were being entered into

the corrective action program with the appropriate significance characterization.

These activities represented seven routine, two local leak rate test (LLRT), and one

containment isolation valve surveillance inspection samples.

25 Enclosure

b. Findings

No findings of significance were identified.

1EP6 Drill Evaluation (71114.06)

a. Inspection Scope

The inspectors observed the licensee perform classifications and protective action

recommendations during licensed operator requalification training on June 20, 2006.

The inspectors observed activities in the control room simulator. The inspectors also

attended the post-drill critique in the simulator. The focus of the inspectors activities

was to note any weaknesses and deficiencies in the shift managers performance as

emergency director and ensure the licensee evaluators noted the same weaknesses

and deficiencies and entered them into the corrective action program. As part of the

inspection, the inspectors reviewed the drill package included in the list of documents

reviewed at the end of this report.

These activities represented one drill evaluation inspection sample.

b. Findings

No findings of significance were identified.

2OS1 Access Control to Radiologically Significant Areas (IP 71121.01)

.1 Plant Walkdowns and Radiation Work Permit Reviews

a. Inspection Scope

The inspectors reviewed licensee controls and surveys in the following three

radiologically significant work areas within radiation areas, high radiation areas and

airborne radioactivity areas in the plant and reviewed work packages which included

associated licensee controls and surveys of these areas to determine if radiological

controls including surveys, postings and barricades were acceptable:

  • Drywell Activities; and
  • Refuel Floor Activities.

These activities represented one inspection sample.

The inspectors reviewed the radiation work permits (RWPs) and work packages used to

access the three areas and other high radiation work areas to identify the work control

instructions and control barriers that had been specified. Electronic dosimeter alarm set

points for both integrated dose and dose rate were evaluated for conformity with survey

indications and plant policy. Workers were interviewed to verify they were aware of the

actions required when their electronic dosimeters noticeably malfunctioned or alarmed.

26 Enclosure

These activities represented one inspection sample.

The inspectors walked down and surveyed (using an NRC survey meter) the three areas

to verify the prescribed RWPs, procedure, and engineering controls were in place,

licensee surveys and postings were complete and accurate, and air samplers were

properly located.

These activities represented one inspection sample.

The inspectors reviewed RWPs for the following airborne radioactivity areas to verify

barrier integrity and engineering controls performance, e.g., high efficiency particulate

air filter ventilation system operation, and to determine if there was a potential for

individual worker internal exposures of greater than 50 millirem committed effective

dose equivalent. There were no areas where there was a potential for individual worker

internal exposures of greater than 50 millirem committed effective dose equivalent.

Work areas having a history of, or the potential for, airborne transuranic isotopes were

evaluated to verify the licensee had considered the potential for transuranic isotopes

and provided appropriate worker protection. There where no areas having a history of,

or the potential for, airborne transuranic isotopes.

These activities represented one inspection sample.

The adequacy of the licensees internal dose assessment process for any actual internal

exposures greater than 50 millirem committed effective dose equivalent was assessed.

There were no internal exposures greater than 50 millirem committed effective dose

equivalent.

These activities represented one inspection sample.

b. Findings

No findings of significance were identified.

.2 Problem Identification and Resolution

a. Inspection Scope

The inspectors reviewed three corrective action reports related to access controls and

high radiation area radiological incidents. Staff members were interviewed and

corrective action documents were reviewed to verify that follow-up activities were being

conducted in an effective and timely manner commensurate with their importance to

safety and risk based on the following:

  • initial problem identification, characterization, and tracking;
  • disposition of operability/reportability issues;
  • evaluation of safety significance/risk and priority for resolution;
  • identification of repetitive problems;
  • identification of contributing causes;
  • identification and implementation of effective corrective actions;

27 Enclosure

  • resolution of NCVs tracked in the corrective action system; and
  • implementation/consideration of risk-significant operational experience feedback.

These activities represented one inspection sample.

b. Findings

No findings of significance were identified.

.3 Job-In-Progress Reviews

a. Inspection Scope

The inspectors observed the following three jobs that were being performed in radiation

areas, airborne radioactivity areas, or high radiation areas for observation of work

activities that presented the greatest radiological risk to workers:

  • Drywell Cooler Number Four Removal;
  • Perform Refuel Activities.

The inspectors reviewed radiological job requirements for the three activities including

RWP requirements and work procedure requirements, and attended As-Low-As-Is-

Reasonably-Achievable (ALARA) job briefings.

These activities represented one inspection sample.

Job performance was observed with respect to these requirements to verify radiological

conditions in the work area were adequately communicated to workers through pre-job

briefings and postings. The inspectors also verified the adequacy of radiological

controls including required radiation, contamination, and airborne surveys for system

breaches; radiation protection job coverage which included audio and visual surveillance

for remote job coverage; and contamination controls.

These activities represented one inspection sample.

b. Findings

No findings of significance were identified.

.4 Radiation Worker Performance

a. Inspection Scope

During job performance observations, the inspectors evaluated radiation worker

performance with respect to stated radiation protection work requirements and

evaluated whether workers were aware of the significant radiological conditions in their

workplace, the RWP controls and limits in place, and that their performance had

accounted for the level of radiological hazards present.

28 Enclosure

These activities represented one inspection sample.

The inspectors reviewed radiological problem reports which found the cause of the

event was due to radiation worker errors to determine if there was an observable pattern

traceable to a similar cause, and to determine if this perspective matched the corrective

action approach taken by the licensee to resolve the reported problems. These

problems, along with planned and taken corrective actions were discussed with the

Radiation Protection Manager.

These activities represented one inspection sample.

b. Findings

No findings of significance were identified.

.5 Radiation Protection Technician (RPT) Proficiency

a. Inspection Scope

During job performance observations, the inspectors evaluated RPT performance with

respect to radiation protection work requirements and evaluated whether they were

aware of the radiological conditions in their workplace, the RWP controls and limits in

place, and if their performance was consistent with their training and qualifications with

respect to the radiological hazards and work activities.

These activities represented one inspection sample.

The inspectors reviewed two radiological problem reports which found the cause of the

event was radiation protection technician error to determine if there was an observable

pattern traceable to a similar cause, and to determine if this perspective matched the

corrective action approach taken by the licensee to resolve the reported problems.

These activities represented one inspection sample.

b. Findings

No findings of significance were identified.

2OS2 As-Low-As-Is-Reasonably-Achievable Planning And Controls (ALARA) (IP 71121.02)

.1 Inspection Planning

a. Inspection Scope

The inspectors reviewed plant collective exposure history, current exposure trends,

ongoing and planned activities in order to assess current performance and exposure

challenges. This included determining the plants current 3-year rolling average for

collective exposure in order to help establish resource allocations and to provide a

perspective of significance for any resulting inspection finding assessment.

29 Enclosure

These activities represented one inspection sample.

The inspectors reviewed the outage work scheduled during the inspection period and

associated work activity exposure estimates for the following five work activities which

were likely to result in the highest personnel collective exposures:

  • Drywell Cooler Number Four Removal;
  • Refuel Floor Activities;
  • In-Service Inspections.

These activities represented one inspection sample.

The inspectors determined site specific trends in collective exposures and source-term

measurements. The inspectors reviewed procedures associated with maintaining

occupational exposures ALARA and processes used to estimate and track work activity

specific exposures.

These activities represented two inspection samples.

b. Findings

No findings of significance were identified.

.2 Radiological Work Planning

a. Inspection Scope

The inspectors evaluated the licensees list of planned work activities for RF11 ranked

by estimated exposure that were in progress and reviewed the following three work

activities of exposure significance:

  • 06-1113, CRD Exchange;
  • 06-1205, East/West MSR Replacement; and
  • 06-1124, Drywell Cooler Number Four Removal.

For these three activities, the inspectors reviewed the ALARA work activity evaluations,

exposure estimates, and exposure mitigation requirements in order to verify the licensee

had established procedures and engineering and work controls that were based on

sound radiation protection principles in order to achieve occupational exposures that

were ALARA. This also involved determining that the licensee had reasonably grouped

the radiological work into work activities, based on historical precedence, industry

norms, and/or special circumstances.

The inspectors compared the results achieved including dose rate reductions and

person-rem used with the intended dose established in the licensees ALARA planning

for these three work activities. Reasons for inconsistencies between intended and

actual work activity doses were reviewed.

30 Enclosure

These activities represented one inspection sample.

b. Findings

No findings of significance were identified.

.3 Verification of Dose Estimates and Exposure Tracking Systems

a. Inspection Scope

The licensees process for adjusting exposure estimates or re-planning work, when

unexpected changes in scope, emergent work or higher than anticipated radiation levels

were encountered, was evaluated. This included determining that adjustments to

estimated exposure (intended dose) were based on sound radiation protection and

ALARA principles and not adjusted to account for failures to control the work. The

frequency of these adjustments was reviewed to evaluate the adequacy of the original

ALARA planning process.

These activities represented one inspection sample.

b. Findings

No findings of significance were identified.

.4 Job Site Inspections and ALARA Control

a. Inspection Scope

The inspectors observed the following five jobs that were being performed in radiation

areas, airborne radioactivity areas, or high radiation areas for observation of work

activities that presented the greatest radiological risk to workers.

  • Drywell Cooler Number Four Removal;
  • Refuel Floor Activities;
  • In-Service Inspections.

The licensees use of engineering controls to achieve dose reductions was evaluated to

verify procedures and controls were consistent with the licensees ALARA reviews,

sufficient shielding of radiation sources was provided for, and the dose expended to

install/remove the shielding did not exceed the dose reduction benefits afforded by the

shielding.

These activities represented one inspection sample.

b. Findings

No findings of significance were identified.

31 Enclosure

.5 Radiation Worker Performance

a. Inspection Scope

Radiation worker and RPT performance was observed during work activities being

performed in radiation areas, airborne radioactivity areas, and high radiation areas that

presented the greatest radiological risk to workers. The inspectors evaluated whether

workers demonstrated the ALARA philosophy in practice by being familiar with the work

activity scope and tools to be used, by utilizing ALARA low dose waiting areas, and that

work activity controls were being complied with. Also, radiation worker training and skill

levels were reviewed to determine if they were sufficient relative to the radiological

hazards and the work involved.

These activities represented one inspection sample.

b. Findings

No findings of significance were identified.

4. OTHER ACTIVITIES (OA)

4OA2 Identification and Resolution of Problems (71152)

.1 Routine Review of Identification and Resolution of Problems

a. Inspection Scope

As discussed in previous sections of this report, the inspectors routinely reviewed issues

during baseline inspection activities and plant status reviews to verify they were being

entered into the licensee's corrective action system at an appropriate threshold,

adequate attention was being given to timely corrective actions, and adverse trends

were identified and addressed.

b. Findings

No findings of significance were identified.

.2 Semi-Annual Trend Review

a. Inspection Scope

The inspectors performed a screening review of each item entered into the licensees

corrective action program to identify trends that might indicate the existence of a more

significant safety issue. The inspectors considered repetitive or closely related issues

that may have been documented by the licensee outside the normal corrective action

program, such as in:

C trend reports or performance indicators,

C major equipment problem lists,

32 Enclosure

C repetitive and/or rework maintenance lists,

C departmental problem/challenges lists,

C system health reports,

C quality assurance audit/surveillance reports,

C self assessment reports,

C maintenance rule assessments, or

C corrective action backlog lists.

The inspectors verified the licensee was identifying issues at an appropriate threshold

and entering them into their corrective action program by comparing those issues

identified by the NRC during the conduct of the plant status and inspectable area

portions of the program with those issues identified by the licensee.

b. Issues

Unidentified drywell leakage was fluctuating after startup from RF11 but has since

leveled out. From the lowest value, unidentified leakage has increased from about

0.06 gpm to an average daily value of 0.14 gpm. Additionally, the inner seal pressure

for the B reactor recirculation pump has been fluctuating by as much as 40-60 psig;

however, there does not appear to be a correlation between the seal pressure

oscillations and drywell leakage. These issues are in the licensees corrective action

program as CARDs 06-24313 for the unidentified leakage and 06-23791 for the seal

pressure oscillations.

4OA3 Event Followup (71153)

.1 Reactor Scram due to Main Transformer Fault

a. Inspection Scope

As described in Section 1R20.3 of this report, the inspectors responded to the control

room on June 15, 2006, when the reactor automatically shut down as a result of the

failure of main unit transformer 2B. The inspectors observed plant parameters and

status, evaluated the performance of mitigating systems and licensee actions, confirmed

that the licensee properly classified the event in accordance with emergency action level

procedures and made timely notifications to NRC and state/county governments, as

required by 10 CFR 50.72 (Event Number 42643). The inspectors determined and

communicated details regarding the event to NRC management, risk analysts and

others in Region III and Headquarters as input to an evaluation per Management

Directive 8.3 for determining the appropriate level of event response. Based on the

events that occurred, routine resident inspection efforts were deemed appropriate.

b. Findings

No findings of significance were identified.

33 Enclosure

.2 Review of Licensee Event Reports (LER)

a. (Closed) LER 50-341/2006-001: At 0039 hours4.513889e-4 days <br />0.0108 hours <br />6.448413e-5 weeks <br />1.48395e-5 months <br /> on April 1, 2006, Fermi 2 feedwater line

check valves B2100F010A and B2100F076A failed their LLRT. The air leakage rate of

the inboard check valve B2100F010A was 324.21 standard cubic feet per hour (SCFH),

and the leakage rate of outboard check valve B2100F076A was above the

measurement capability of the leak rate monitor. The penetration (X-9A) minimum-

pathway air leakage value was determined to be 324.21 SCFH which is greater than the

allowable containment leakage rate (La) value of 296.3 SCFH per TS 5.5.12 and higher

than the allowable secondary containment bypass leakage rate of 0.1 La or 29.63 SCFH

per TS Surveillance Requirement 3.6.1.3.11. The B2100F076A failure was attributed to

soft seat degradation which was primarily caused by extending its service time to three

operating cycles. The B2100F010A valve failure was attributed to soft seat degradation

due to a slight misalignment of the valve disc to the in-body seat, compounded by wear

between the internal shaft and valve disc. The slight misalignment caused the soft seat

along the top portion of the disc to contact the seat first, resulting in a scraping action as

the disc flexed to its full seat position. For both valves, the soft seats were replaced,

and the soft seat service time has been limited to two operating cycles. The internal

shaft for the B2100F010A valve was replaced, and the alignment between the disc and

the valve seat was adjusted. Both valves were retested and met their associated LLRT

acceptance criteria prior to restart of the unit.

The LER was reviewed by the inspectors. No findings of significance were identified

and no violation of NRC requirements occurred. The licensee documented the LLRT

failure in CARD 06-21751. This LER is closed.

4OA6 Exit Meetings

.1 Exit Meeting Summary

On July 11, 2006, the inspectors presented the inspection results to Mr. D. Cobb and

other members of licensee management at the conclusion of the inspection. The

inspectors asked the licensee whether any material examined during the inspection

should be considered proprietary. No proprietary information was identified.

.2 Interim Exit Meetings

On April 7, 2006, an interim exit meeting was conducted for the Access Control to

Radiological Areas and ALARA inspection with Mr. Kevin Hlavaty, Plant Manager, and

other licensee staff.

4OA7 Licensee-Identified Violations

The following violation of very low significance was identified by the licensee and is a

violation of NRC requirements, which meet the criteria of Section VI of the NRC

Enforcement Manual, NUREG-1600, for being dispositioned as an NCV.

34 Enclosure

Cornerstone: Public Radiation Safety

The licensees procedure 67.000.103, Surveying of Outgoing Shipments, directs the

staff to survey outgoing vehicles used to carry an exclusive use shipment of radioactive

material. The procedure relies on the proper identification of the incoming shipment as

an exclusive use shipment. This procedure is used to implement the requirements of

49 CFR 173.443 and 49 CFR 177.843 that require the specific release survey of

vehicles in exclusive use situations. Contrary to the above, and as described in

CARD 06-21389, on March 20, 2006, an exclusive use radioactive material shipment

was received by the licensee. The shipment contained one package of Limited Quantity

radioactive material and four boxes of non-radioactive material and the radiation

protection staff assigned to accept the shipment incorrectly identified the shipment as a

non-exclusive use shipment. After the packages were removed from the conveyance,

the vehicle was released without the required survey. This was identified by licensee

supervision but not before the vehicle had departed the site. The carrier was contacted

and the vehicle returned to the licensees site before further transportation activity had

commenced and a survey was completed. No contamination was found and no dose

rates above background were identified. The finding is of very low safety significance

because it did not result in an unmonitored release nor were any dose limits

approached.

ATTACHMENT: SUPPLEMENTAL INFORMATION

35 Enclosure

KEY POINTS OF CONTACT

Licensee

D. Gipson, Chief Nuclear Officer

D. Cobb, Assistant Vice President, Nuclear Generation

K. Hlavaty, Plant Manager

S. Bartman, Nuclear Production

J. Davis, Manager, Outage Management

R. Gaston, Licensing Manager

S. Hassoun, Principal Engineer, Licensing

H. Higgins, Radiation Protection Manager

J. Korte, Manager, Nuclear Security

J. Plona, Engineering Director

NRC

C. Lipa, Chief, Division of Reactor Projects, Branch 4

1 Attachment

LIST OF ITEMS OPENED, CLOSED, AND DISCUSSED

Opened

05000341/2006003-05 URI Inappropriate Use of Risk in Operability Evaluations

(Section 1R15.3)

Opened and Closed

05000341/2006003-01 NCV Unauthorized Transient Combustibles in Safety-Related

Areas (Section 1R05.2)05000341/2006003-02 NCV Improper Storage of Chemicals Affecting Fire Fighting

Response (Section 1R05.3)05000341/2006003-03 NCV Inadequate Maintenance Risk Assessment

(Section 1R13.2)05000341/2006003-04 NCV Improper Evaluation of Standby Liquid Control Operability

During Tank Sparging (Section 1R15.2)05000341/2006003-06 NCV Inadequate Controls for Venting the Reactor Pressure

Vessel Head (Section 1R20.1)

Closed

05000341/2006-001 LER Excessive Feedwater Check Valve Leakage at Containment

Penetration

Discussed

None.

2 Attachment

LIST OF DOCUMENTS REVIEWED

The following is a list of documents reviewed during the inspection. Inclusion on this list does

not imply that the NRC inspectors reviewed the documents in their entirety but rather that

selected sections of portions of the documents were evaluated as part of the overall inspection

effort. Inclusion of a document on this list does not imply NRC acceptance of the document or

any part of it, unless this is stated in the body of the inspection report.

1R01: Adverse Weather Protection

CARD 06-23861, 06/05/06; Procedure Enhancement for TBHVAC (NRC Comment)

Procedure 27.000.06, Rev 0, 02/27/03; Performance Evaluation Procedure, Hot Weather

Operations

Open/Closed Work Requests by Related Work Code; 05/04/06

1R04: Equipment Alignment

Drawing 6M721-5706-3, 2/16/00; RHR Service Water Make Up Decant and Overflow Systems

Functional Operating Sketch

Drawing 6M721-5706-1, 3/5/04; Residual Heat Removal (RHR) Division II Functional Operating

Sketch

03-00120, 01/02/03; Pinhole leak in piping

03-13694, 6/17/03; Document the Condition of General Service Water Piping

04-24918, 10/25/04; P4100F402A installed at the bottom of the pipe

06-11615, 05/19/06; EDG Electrical Lineup Load Description Changes

06-21618, 03/28/06; E1100F050A Failed PI Leak Test SR 3.4.5.1

06-22730, 4/24/06; NRC-Identified Concerns in GSW Pumphouse

06-23447, 05/18/06; 23.205 Att 1B enhancement

06-23494, 05/20/06; E1100F050A actuator failed to open valve

23.131, Rev.86; General Service Water System

43.000.005, Rev. 30; Visual Examination of Piping and Components (VT-2)

23.208, Rev. 81; RHR Complex Service Water Systems

23.205, Rev. 94; Residual Heat Removal System

1R05: Fire Protection

CARD 06-23365; Door is not latching; Dated May 15, 2006 (NRC-Identified)

CARD 06-23388; Transient Combustibles in the RHR; Dated May 16, 2006 (NRC-Identified)

MOP11; Fire Protection; Revision 10

Fire Brigade Drill Scenario 6, Rev. 11/29/94; First Floor Radioactive Waste Chemical Lab

Storage Area

Fire protection Pre-Plan FP-RDWST, Rev. 4; Radwaste Building Zones 22, 23, 24, and 25

1R06: Flood Protection Measures

CARD 06-21354; High Pressure Coolant Injection Room Flooded due to Drains backing Up;

3/18/06

CARD 06-22600; Moderate Energy Line Break Evaluation; 4/21/06 (NRC-Identified)

3 Attachment

Nuclear Generation Memo TMPE-94-0308; May 18, 1994; Flood Protection Review

6M721-2223, Rev U, 11/24/06; Diagram Equipment Drains All Floors Auxiliary and Reactor

Buildings

6M721-2224, Rev W, 11/24/04; Diagram Floor Drains All Floors Auxiliary and Reactor Buildings

6M721-2032, Rev BO, 04/19/06; Sump Pump Diagram Radwaste System

6M721-2032-1, Rev AI, 04/19/06; Sump Pump Diagram Radwaste System

1R07: Heat Sink Performance

WR TG25060421; Perform RHR Division II Heat Exchanger Performance Test; 3/22/06

1R11: Licensed Operator Requalification

Scenario SS-OP-802-3300, Rev. 0; Anticipated Transient Without Scram with Small Steam

Leak; 1/26/06

1R12: Maintenance Effectiveness

Design Specification 3071-128-EZ-06; Electrical Design Instructions Molded Case Circuit

Breakers

Maintenance Rule Conduct Manual MMR, Appendix E, Rev 4; Maintenance Rule SSC Specific

Functions

Memo dtd 01/30/06, TMIS-06-0011; Summary of Expert Panel Meeting 184 Conducted

January 24, 2006

CTG11-1 Get Well Plan; July 2003

Deviation Event Report 93-0528, 09/15/93

Vendor Manual VME5-18, Rev 0; Spectrum Technologies, Series 5600, MCC

CARD 97-10182, 10/27/97; Defective Molded Case Circuit Breaker

CARD 03-01098,05/30/03; Reactor Protection System - Function Failure

03-19510,07/20/03; Safety Eval 95-0002 is Used as an Operability Evaluation for LPCI with the

RHR Minimum Flow Valves Open

CARD 04-22685, 07/02/04; Generator Transformer - Function Failure

CARD 04-23307. 08/03/04; Motor Control Centers & Dist. Cabinets

CARD 05-23490, 06/21/05; Auxiliary Electrical - Function Failure

CARD 06-21363, 04-02-06; Auxiliary Electrical - Function Failure

CARD 06-21527, 04/09/06; Residual Heat Removal System - Function Failure

CARD 06-22270, 04/12/06, Maintenance Rule Function T4100-09 should be included in

Maintenance Rule Scope Investigation

Procedure 35.306.008, Rev 46; Maintenance Procedure, ITE Gould Motor Control Center Load

Compartment

Procedure 35.306.018, Rev 5; Maintenance Procedure, Spectrum Technology Motor Control

Center Load Compartment

1R13: Maintenance Risk Assessment and Emergent Work Evaluation

Fermi 2 Daily Plant Status, April 2, 2006

Schedulers Evaluation for Fermi 2, April 2, 2006

Fermi 2 Daily Plant Status, April 17, 2006

Schedulers Evaluation for Fermi 2, April 17, 2006

4 Attachment

Fermi 2 Daily Plant Status, April 30, 2006

Schedulers Evaluation for Fermi 2, April 30, 2006

Fermi 2 Daily Plant Status, June 26, 2006

Schedulers Evaluation for Fermi 2, June 26, 2006

CARD 06-21892, 4/4/06; NRC Questions related to Temporary Cooling Installed for Division I

Battery Test (NRC-Identified)

CARD 06-24495, 7/7/06; Work Risk Assessment and Temporary Equipment Controls

(NRC-Identified)

WR 0219060414; Perform 42.309.05 Division I (5 Year) 130/260 VDC batter Check (2A-1 Only)

WR 1219060414; Perform 42.309.05 Division I (5 Year) 130/260 VDC batter Check (2A-2 Only)

1R14: Non-Routine Events

CARD 06-24113; Main Steam Bypass Valves Opened Unintentionally During Power Ascension;

6/18/06

CARD 06-23588; Mode 5 Reactor SCRAM During Installation of SRM Shorting Links; 5/24/06

CARD 06-23501; Full In Light for Control Rod 50-27 on Full Core Display is Intermittent;

5/20/06

1R15: Operability Evaluations

Drawing - 5744, Rev. BK; Emergency Equipment Cooling Water Division I; 11/23/05

WR 000Z060107; Remove and Reinstall Insulation on E1100F031B; 2/9/06

WR 000Z062027; Replace Contaminated Insulation; 6/12/06

CARD 06-24156; Affects of Accidents not Addressed in Insulation Removal Evaluation for

E1100F031B; 6/20/06 (NRC Identified)

CARD 01-17302; There are no Site Guidelines for Insulation Removal on Operable Equipment;

8/14/01

CARD 06-23898; EECW M/U Pump IST Flow Unattainable; 6/7/06

CARD 02-14782; Engineering Evaluation for On-Line Insulation Removal; 6/27/02

CARD 03-16498; Engineering Evaluation for On-Line Insulation Removal; 9/9/03

CARD 05-21940; Engineering Evaluation for On-Line Insulation Removal; 3/23/05

CARD 06-23913; Replace Contaminated Insulation; 6/8/06

CARD 06-23785; Standby Liquid Control Operability During Sparging Activities; 6/1/06 (NRC-

Identified)

CARD 99-13240; Inoperability of Standby Liquid Control During Air Sparging; 4/15/99

1R19: Post-Maintenance Testing

EDP - 31880 120 KV Switchyard Upgrade

Engineering Change Request 33690-1, Rev A, 03/14/06; Replacement of Drywell Cooler Coils

T470B003 and T4700B004

Equivalent Replacement Evaluation (ERE) 34173, Rev 0, 04/18/06; E1150F608 MOV Motor

Replacement

Oil Sample Analysis Reports for C1106C001A, E Control Rod Drive Pump; 01/01/06 -

06/29/06

CARD 06-22258, 04/12/06; CTG equipment issues discovered during IPTE 04-02

CARD 06-22982, 4/30/06; Inboard MSIV A will not slow close

CARD 06-23031, 5/1/06; MSIV B2103F028B RPS Limit Switch did not actuate when expected

5 Attachment

CARD 06-22634, 4/22/06; A Inboard MSIV limit switch, PIS B21N572A, will not change state

Drawing SD-F-0179, Rev. A, 9/25/05; Diagram Line Breaker Control 120KV, POS GK

Drawing SD-2500-01, Rev. A, 2/28/06; One Line Diagram Plant 4160V & 480V

Drawing SD-2500-02, Rev. A, 2/23/06; One Line Diagram 13.8KV

Drawing SD-F-0001, Rev. A, 2.23/06; One Line Diagram 120 KV Switchyard

IPTE 04-02, 120KV Switchyard Upgrade

Procedure 24.137.01, Rev. 34; Main Steam Isolation Channel Functional Test

24.206.01, Rev 63, 05/08/06; RCIC System Pump and Valve Operability Test

43.000.005, Rev 30, 03/22/06; Visual Examination of Piping and Components (VT-2)

43.401.303, Rev 32, 10/24/05; Local Leakage Rate Testing for Penetration X-9A

WR B203040100, 04/10/06; B2100F010A - Nuclear Boiler Feedwater Supply Inboard Primary

Containment Check Valve

WR 000Z050487, 04/29/06;B3105F031A - Reactor Recirculation Pump A Discharge Valve

WR T210040100, 04/10/06; B2100F076A - Nuclear Boiler Feedwater Supply Check Valve

WR 000Z052131, 04/19/06; Inservice Testing, Drywell Cooler #4

WR 000Z060156, 6/19/06; E Control Rod Drive Inboard Pump Bearing Oil level Bulls eye Dirty

1R20: Refueling and Outage Activities

Apparent Cause Determination for Damage Found in the Main Generator During RF11 Robot

Inspections CARD 06-21922

Inspection Requirement Form, Requisition Number: 9086929; 04/19/2006

Drawing 6M721-3722, Rev A; Flow Diagram & Details of Purging Unit - Reactor Pressure

Vessel - Unit 2

Safety Tagging Record 2006-002089

CARD 06-21534, 03/26/2006; Continuous Air Monitor Alarm on Refueling Floor

CARD 06-22590, 04/21/2006; NRC identified concern with Div 1 Core Spray and Defense in

Depth Investigation

CARD 06-22642, 04/22/2006; Are EDG Surveillances Testing What They Are Setup to Test

CARD 06-22667, 04/23/2006; RPV Venting Unit Configuration Control Discrepancies

CARD 06-23114, 05/03/2006; NRC Concern: Review of ERE-34173 E1150F608 MOV Motor

Replacement

CARD 06-23793, 06/02/2006; NRC Concern - Material Released Without the Requirements of

EED Being Verified

Procedure 24.106.06, Rev 25; Surveillance Procedure, SCRAM Discharge Volume Vent and

Drain Valves SCRAM Operability Test

Procedure 32.000.07, Rev 33; Crane Operation Procedure, Reactor Building Crane Operation

Procedure 35.717.001, Rev 29; Maintenance Procedure, Reactor Building Crane - Quarterly

Preventive Maintenance

Procedure 35.717.003, Rev 3; Maintenance Procedure, Reactor Building Crane - Annual PM

Inspection

Procedure 43.401.303, Rev 32; Surveillance Procedure, Local Leakage Rate Testing for

Penetration X-9A

Work Control Conduct Manual MWC13, Rev 0; Outage Nuclear Safety

Maintenance Conduct Manual MMA07, Rev 14; Hoisting, Rigging and Load Handling

6 Attachment

1R22: Surveillance Testing

Drawing 6M721-5703-1, Rev. Y; Control Rod Drive System Functional Operating Sketch

CARD 06-22739, 4/24/06; Acrid smell from EDG #13 local control cabinet

CARD 06-23031, 5/1/06; MSIV B2103F028B RPS Limit Switch did not actuate when expected

CARD 06-22653, 04/23/06; HCU 46-27 Conduit for wiring to accumulator pressure switch

needs repair

CARD 06-22999, 05/01/06; Enhancements to 24.405.03

CARD 06-21681; Potential Enhancement for MSIV Switch Calibrations; 3/20/06 (NRC-

Identified)

CARD 06-21720; NRC Question Regarding MSIV Switch Testing; 3/31/06 (NRC-Identified)

CARD 06-22046; Loss of SLC Squib Valve A Continuity Light During Performance of

24.139.03; 4/7/06

Procedure 24.106.06, Rev 25; Surveillance Procedure, SCRAM Discharge Volume Vent and

Drain Valves SCRAM Operability Test

Procedure 24.106.08, Rev. 3; CRD Hydraulic Unit Accumulator Integrity Test

Procedure 24.137.01, Rev. 34; Main Steam Isolation Channel Functional Test

Procedure 24.405.03, Rev. 33; Secondary Containment Operability Test

Procedure 24.307.03, Rev. 38; EDG 13 - Loss of Offsite Power and ECCS Start with Loss of

Offsite Power Test

Procedure 24.202.02, Rev. 42; HPCI Flow Rate Test at 165 psig Reactor Steam Pressure

Procedure 24.206.04, Rev. 44; RCIC System Automatic Actuation and Flow Test

Procedure 43.401.500, Rev 34; Surveillance Procedure, Local Leakage Rate Testing for

Penetration X-7A, X-7B, X-7C, and X-7D

Procedure 43.401.500, Rev 35; Surveillance Procedure, Local Leakage Rate Testing for

Penetration X-7A, X-7B, X-7C, and X-7D

Procedure 24.402.06; Rev. 32; Drywell to Suppression Chamber Bypass Leak Test

Procedure 35.139.002; Rev. 27; SLC System Explosive Valve Insert Replacement

Procedure 24.139.03, Rev. 40; SLC Manual Initiation, RWCU Isolation, and Storage tank

Heater Operability Test

WR 0311060425; Perform 24.402.06 Drywell to Suppression Chamber Bypass Leak Test;

3/25/06

WR 0518041022; Perform 44.010.063 RPS MSIV Outboard Valve Limit Switch, Div. I and II,

Calibration

WR 1245060421; Perform 24.139.03 SLC Loop B Pump Flow, Manual Initiate, and Squib

Firing; 4/21/06

1EP6: Drill Evaluation

Scenario SS-OP-802-3300, Rev. 0; Anticipated Transient Without Scram with Small Steam

Leak; 1/26/06

2OS1: Access Control to Radiologically Significant Areas

CARD 05-26818; Primary Containment Atmosphere Sample Pump; T5001-C003 Will Not Start;

dated December 5, 2005

CARD 06-11546; WGI Employee Felt Something in His Left Eye after Removing Protective

Clothing at Drywell Step-off Pad; dated April 5, 2006

CARD 06-21534; High Radiation Alarm on Refuel Floor; dated March 26, 2006

7 Attachment

CARD 06-21640; Unnecessary Contamination of Personnel; dated March 29, 2006

CARD 06-21639; Evaluate Dose an Dose Rate Alarms for Fast Entry Electronic Dosimeters;

dated March 29, 2006

CARD 06-20962; Worker Electronic Dosimeter Alarm on Incorrect Task; dated February 23,

2006

CARD 06-21177; Unexpected Dose Rate Alarm; dated March 8, 2006

CARD 06-21787; Entering High Radiation Area on Incorrect Task; dated April 1, 2006

CARD 06-21807; Evaluate Reactor Building Ventilation Impact on the Spread of Contamination

during RF11 Vessel Fill Up; dated April 2, 2006

CARD 06-21857; Drywell Stepoff Pad Poor Radiation Protection Practices; dated April 3, 2006

CARD 06-21873; Potential Release of Radioactive Contamination; dated April 4, 2006

CARD 06- 21868; Workers Entered Top of Torus High Radiation Area on Wrong Radiation

Work Permit; dated April 4, 2006

CARD 06-21944; Foreign Material Found Inside Main Condenser Upper Steam Space; dated

April 5, 2006

CARD 06-21958; Worker Received Puncture Wound; dated April 6, 2006

EP-225; Radiological Medical Emergencies; Revision 13

RF11 ALARA Self-Assessment; dated April 4, 2006

2OS2 As-Low-As-Is-Reasonably-Achievable Planning And Controls (ALARA)

RWP 06-1110; In-Service Inspections; Revision 0

RWP 06-1103; Install and Remove Temporary Shielding, Install Permanent Shielding;

Revision 0

RWP 06-1105; Job Progress for Scaffold Activities in the Reactor Building Steam Tunnel and

Drywell; Revision 0

RWP 06-1124; Replace Number 4 Drywell Cooler; Revision 4

RWP 06-1164; E1100F031A Cutout and Replace Check Valve; Revision 0

RWP 06-1251; Perform Refuel Activities on Reactor Building 5; Revision 0

CARD 06-21765; Work Initiated Without Radiation Protection Review; dated April 1, 2006

CARD 06-21911; E100F031A Glovebag Not Installed Properly; dated April 5, 2006

CARD 06-21947; E1100F060A Re-pack Extra Time and Dose Above Initial Estimate; dated

April 5, 2006

Procedure 63.000.100; Respirator Evaluation Work Sheet (RWP 06-1117); Revision 0

4OA2: Identification and Resolution of Problems

CARDs initiated between 1/1/06 and 06/30/06

4OA3: Event Followup (71153)

NRC-06-0037 Letter; Licensee Event report No. 2006-001, Excessive Feedwater Check Valve

Leakage At Containment Penetration; dated May 24, 2006

4OA7 Licensee-Identified Violations

CARD 06-21389; Failure to Perform Required Surveys in Accordance with

Procedure 67.000.102; dated March 21, 2006

Procedure 67.000.103; Survey of Outgoing Radioactive Material Shipments; Revision 16

Procedure 67.000.102; Survey of Incoming Radioactive Material Shipments; Revision 0

8 Attachment

LIST OF ACRONYMS USED

ALARA As Low As Reasonable Achievable

CARD Condition Assessment Resolution Document

CDF Core Damage Frequency

CFR Code of Federal Regulations

CTG Combustion Turbine Generator

DRP Division of Reactor Projects

EDG Emergency Diesel Generator

GSW General Service Water

HPCI High Pressure Coolant Injection

IMC Inspection Manual Chapter

LER Licensee Event Report

LERF Large Early Release Frequency

LLRT Local Leak Rate Test

MCC Motor Control Center

MSIV Main Steam Isolation Valve

NCV Non-Cited Violation

NRC Nuclear Regulatory Commission

PI Performance Indicator

PMT Post-Maintenance Testing

RCIC Reactor Core Isolation Cooling

RCS Reactor Coolant System

RHR Residual Heat Removal

RHRSW Residual Heat Removal Service Water

RPS Reactor Protection System

RPSMG Reactor Protection System Motor Generator

RPT Radiation Protection Technician

RWCU Reactor Water Cleanup

RWP Radiation Work Package

SCFH Standard Cubic Feet Per Hour

SCFM Standard Cubic Feet Per Minute

SDP Significance Determination Process

SGTS Standby Gas Treatment System

SLC Standby Liquid Control

SPAR Standardized Plant Analysis Risk

SRA Senior Reactor Analyst

TM Temporary Modifications

TS Technical Specifications

UFSAR Updated Final Safety Analysis Report

WR Work Request

9 Attachment