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{{#Wiki_filter:UNITED STATES NUCLEAR REGULATORY COMMISSION REGION I 2100 RENAISSANCE BLVD. KING OF PRUSSIA, PA 19406-2713  
{{#Wiki_filter:UNITED STATES
  August 30, 2016  
                          NUCLEAR REGULATORY COMMISSION
                                          REGION I
Mr. Anthony J. Vitale  
                                  2100 RENAISSANCE BLVD.
Site Vice President Entergy Nuclear Operations, Inc. Indian Point Energy Center  
                                KING OF PRUSSIA, PA 19406-2713
                                          August 30, 2016
Mr. Anthony J. Vitale
Site Vice President
Entergy Nuclear Operations, Inc.
Indian Point Energy Center
450 Broadway, GSB
P.O. Box 249
Buchanan, NY 10511-0249
SUBJECT:        INDIAN POINT NUCLEAR GENERATING - INTEGRATED INSPECTION
                REPORT 05000247/2016002 AND 05000286/2016002
Dear Mr. Vitale:
On June 30, 2016, the U.S. Nuclear Regulatory Commission (NRC) completed an inspection at
your Indian Point Nuclear Generating (Indian Point), Units 2 and 3. The enclosed inspection
report documents the inspection results, which were discussed on August 4, 2016, with Larry
Coyle and other members of your staff. Based on additional information provided, the
inspectors conducted an updated exit meeting on August 30, 2016 with John Kirkpatrick, Plant
Operations General Manager and other members of your staff.
The inspection examined activities conducted under your license as they relate to safety and
compliance with the Commissions rules and regulations and with the conditions of your license.
The inspectors reviewed selected procedures and records, observed activities, and interviewed
personnel.
This report documents three NRC-identified findings of very low safety significance (Green).
These findings involved violations of NRC requirements. However, because of the very low
safety significance, and because they are entered into your corrective action program, the NRC
is treating these findings as non-cited violations, consistent with Section 2.3.2.a of the NRC
Enforcement Policy. If you contest any non-cited violation in this report, you should provide a
response within 30 days of the date of this inspection report, with the basis for your denial, to
the Nuclear Regulatory Commission, ATTN: Document Control Desk, Washington, DC
20555-0001; with copies to the Regional Administrator, Region I; the Director, Office of
Enforcement, U.S. Nuclear Regulatory Commission, Washington, DC 20555-0001; and the
NRC Senior Resident Inspector at Indian Point. In addition, if you disagree with the
cross-cutting aspect assigned to any finding in this report, you should provide a response within
30 days of the date of this inspection report, with the basis for your disagreement, to the
Regional Administrator, Region I, and the NRC Senior Resident Inspector at Indian Point.


450 Broadway, GSB
A. Vitale                                       -2-
P.O. Box 249
In accordance with Title 10 of the Code of Federal Regulations (10 CFR) 2.390 of the NRCs
 
Rules of Practice, a copy of this letter, its enclosure, and your response (if any) will be
Buchanan, NY 10511-0249
available electronically for public inspection in the NRCs Public Document Room or from the
 
Publicly Available Records component of the NRCs Agencywide Documents Access and
SUBJECT: INDIAN POINT NUCLEAR GENERATING - INTEGRATED INSPECTION REPORT 05000247/2016002 AND 05000286/2016002
Management System (ADAMS). ADAMS is accessible from the NRC website at
http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room).
Dear Mr. Vitale:
                                                  Sincerely,
 
                                                  /RA/
On June 30, 2016, the U.S. Nuclear Regulatory
                                                  Glenn T. Dentel, Chief
Commission (NRC) completed an inspection at your Indian Point Nuclear Generating (Indian Point), Units 2 and 3.  The enclosed inspection report documents the inspection results, which were discussed on August 4, 2016, with Larry
                                                  Reactor Projects Branch 2
Coyle and other members of your staff.  Based on additional information provided, the
                                                  Division of Reactor Projects
inspectors conducted an updated exit meeting on August 30, 2016 with John Kirkpatrick, Plant Operations General Manager and other members of your staff. 
Docket Nos. 50-247 and 50-286
License Nos. DPR-26 and DPR-64
The inspection examined activities conducted under your license as they relate to safety and compliance with the Commission's rules and regulations and with the conditions of your license. 
Enclosure:
The inspectors reviewed selected procedures and records, observed activities, and interviewed
Inspection Report 05000247/2016002 and 05000286/2016002
 
   w/Attachment: Supplementary Information
personnel.
cc w/encl: Distribution via ListServ
This report documents three NRC-identified findings of very low safety significance (Green).  These findings involved violations of NRC requirement
s.  However, because of the very low safety significance, and because they are entered into your corrective action program, the NRC
is treating these findings as non-cited violations, consistent with Section 2.3.2.a of the NRC Enforcement Policy.  If you contest any non-cited violation in this report, you should provide a response within 30 days of the date of this inspection report, with the basis for your denial, to
the Nuclear Regulatory Commission, ATTN:  Document Control Desk, Washington, DC
20555-0001; with copies to the Regional Administrator, Region I; the Director, Office of
Enforcement, U.S. Nuclear Regulatory Commission, Washington, DC 20555-0001; and the
NRC Senior Resident Inspector at Indian Point.  In addition, if you disagree with the cross-cutting aspect assigned to any finding in this report, you should provide a response within 30 days of the date of this inspection report, with the basis for your disagreement, to the
Regional Administrator, Region I, and the NRC Senior Resident Inspector at Indian Point.
 
 
A. Vitale -2-  
In accordance with Title 10 of the Code of Federal Regulations (10 CFR) 2.390 of the NRCs "Rules of Practice," a copy of this letter, its enclosure, and your response (if any) will be  
available electronically for public inspection in the NRC's Public Document Room or from the Publicly Available Records component of the NRC's Agencywide Documents Access and  
Management System (ADAMS). ADAMS is accessible from the NRC website at http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room).  
      Sincerely,       /RA/  
        Glenn T. Dentel, Chief       Reactor Projects Branch 2  
      Division of Reactor Projects  
 
Docket Nos. 50-247 and 50-286 License Nos. DPR-26 and DPR-64  
Enclosure:  
Inspection Report 05000247/2016002 and 05000286/2016002  w/Attachment: Supplementary Information  
cc w/encl: Distribution via ListServ




  ML16243A245
  ML16243A245
  SUNSI Review
                                              Non-Sensitive                             Publicly Available
  Non-Sensitive Sensitive
      SUNSI Review
Publicly Available Non-Publicly Available  
                                              Sensitive                                  Non-Publicly Available
OFFICE RI/DRP RI/DRP RI/DRS RI/DRP RI/DRP  
  OFFICE         RI/DRP               RI/DRP                 RI/DRS               RI/DRP                   RI/DRP
NAME BHaagensen/bh  
                  BHaagensen/bh
NFloyd/nf MGray/mg GDentel/gtd MScott/dlp for DATE 8/29/16 8/24/16 8/30/16 8/30/16 8/30/16  
  NAME                                  NFloyd/nf             MGray/mg             GDentel/gtd             MScott/dlp for
  DATE           8/29/16               8/24/16               8/30/16             8/30/16                 8/30/16
1 Enclosure U.S. NUCLEAR REGULATORY COMMISSION  
                                           
REGION I Docket Nos.  50-247 and 50-286  
                                      1
              U.S. NUCLEAR REGULATORY COMMISSION
                                  REGION I
License Nos. DPR-26 and DPR-64  
Docket Nos.  50-247 and 50-286
 
License Nos. DPR-26 and DPR-64
  Report Nos.  05000247/2016002 and 05000286/2016002  
Report Nos.  05000247/2016002 and 05000286/2016002
 
Licensee:   Entergy Nuclear Northeast (Entergy)
Facility:   Indian Point Nuclear Generating Units 2 and 3
Location:   450 Broadway, GSB
Licensee: Entergy Nuclear Northeast (Entergy)  
            Buchanan, NY 10511-0249
 
Dates:       April 1, 2016, through June 30, 2016
Facility: Indian Point Nuclear Generating Units 2 and 3  
Inspectors:  B. Haagensen, Senior Resident Inspector
 
            G. Newman, Resident Inspector
            S. Rich, Resident Inspector
Location: 450 Broadway, GSB   Buchanan, NY 10511-0249  
            S. Galbreath, Reactor Inspector
 
            J. Furia, Senior Health Physicist
            N. Floyd, Senior Project Engineer
            K. Mangan, Senior Reactor Inspector
Dates:   April 1, 2016, through June 30, 2016  
            J. Poehler, Senior Materials Engineer
 
Approved By: Glenn T. Dentel, Chief
  Inspectors:  B. Haagensen, Senior Resident Inspector  
            Reactor Projects Branch 2
  G. Newman, Resident Inspector  
            Division of Reactor Projects
  S. Rich, Resident Inspector  
                                                          Enclosure
  S. Galbreath, Reactor Inspector J. Furia, Senior Health Physicist N. Floyd, Senior Project Engineer  
K. Mangan, Senior Reactor Inspector  
J. Poehler, Senior Materials Engineer  
Approved By: Glenn T. Dentel, Chief   Reactor Projects Branch 2  
  Division of Reactor Projects  
 
2  TABLE OF CONTENTS SUMMARY ...............................................................................................................................
..... 3REPORT DETAILS ................................................................................................................
....... 51.REACTOR SAFETY .............................................................................................................. 51R04Equipment Alignment .................................................................................................. 51R05Fire Protection ............................................................................................................. 61R07Heat Sink Performance ............................................................................................... 71R08Inservice Inspection Activities ..................................................................................... 71R11Licensed Operator Requalification Program ............................................................... 81R12Maintenance Effectiveness ....................................................................................... 101R13Maintenance Risk Assessments and Emergent Work Control .................................. 131R15Operability Determinations and Functionality Assessments ..................................... 141R18Plant Modifications .................................................................................................... 191R19Post-Maintenance Testing ........................................................................................ 201R20Refueling and Other Outage Activities ...................................................................... 211R22Surveillance Testing .................................................................................................. 241EP6Drill Evaluation .......................................................................................................... 252.RADIATION SAFETY .......................................................................................................... 252RS1Radiological Hazard Assessment and Exposure Controls ........................................ 252RS2Occupational As Low As Is Reasonably Achievable (ALARA) Planning and Controls .............................................................................................................. 262RS7Radiological Environmental Monitoring Program (REMP) ........................................ 264.OTHER ACTIVITIES ............................................................................................................ 2
74OA1Performance Indicator Verification ............................................................................ 274OA2Problem Identification and Resolution ....................................................................... 284OA3Follow Up of Events and Notices of Enforcement Discretion .................................... 344OA5Other Activities .......................................................................................................... 374OA6Meetings, Including Exit ............................................................................................ 39SUPPLEMENTARY INFORMATION ........................................................................................ A-1KEY POINTS OF CONTACT .................................................................................................... A-1LIST OF ITEMS OPENED, CLOSED, DISCUSSED, AND UPDATED ..................................... A-2LIST OF DOCUMENTS REVIEWED ........................................................................................ A-3LIST OF ACRONYMS .............................................................................................................
A-12 
3  SUMMARY  Inspection Report 05000247/2016002 and 05000286/2016002; 04/01/2016 - 06/30/2016; Indian Point Nuclear Generating (Indian Point), Units 2 and 3; Operability Determinations and Functionality Assessments, Refueling and Other Outage Activities, and Follow Up of Events and
Notices of Enforcement Discretion.
 
This report covered a three-month period of inspection by resident inspectors and announced
inspections performed by regional inspectors.  The inspectors identified three findings of very low safety significance (Green), which were non-cited violations (NCVs).  The significance of most findings is indicated by their color (i.e., greater than Green, or Green, White, Yellow, Red)
and determined using Inspection Manual Chapter (IMC) 0609, "Significance Determination
Process," dated April 29, 2015.  Cross-cutting aspects are determined using IMC 0310,
"Aspects within the Cross-Cutting Areas," dated December 4, 2014.  All violations of U.S. Nuclear Regulatory Commission (NRC) requ
irements are dispositioned in accordance with
the NRC's Enforcement Policy, dated February 4, 2015.  The NRC's program for overseeing the
safe operation of commercial nuclear power reactors is described in NUREG-1649, "Reactor Oversight Process," Revision 6.
 
Cornerstone:  Mitigating Systems
  Green.  The inspectors identified a Green NCV of 10 CFR 50, Appendix B, Criterion V, "Instructions, Procedures, and Drawings," because Entergy did not adequately accomplish the actions prescribed by procedure EN-OP-104, "Operability Determination Process," for a
degraded condition associated with the Unit 3 baffle-former bolts.  Specifically, Entergy
incorrectly concluded that no degraded or non-conforming condition existed related to the
Unit 3 baffle-former bolts and exited the operability determination procedure.  Entergy subsequently performed the remaining steps in the procedure and provided appropriate justification for their plans to examine the baffle-former bolts at the next Unit 3 refueling
outage (RFO).  Entergy's immediate corrective actions included entering the issue into its
corrective action program (CAP) as CR-IP3-2016-01961 and documenting an operability
evaluation to support the basis for operability of the baffle-former bolts and the emergency core cooling system (ECCS). This performance deficiency is more than minor because it was associated with the
equipment performance attribute of the Mitigating Systems cornerstone and affected the
cornerstone objective to ensure the availability, reliability, and capability of systems that
respond to initiating events to prevent undesirable consequences (i.e., core damage).  In accordance with IMC 0609.04, "Initial Characterization of Findings," and Exhibit 2 of IMC 0609, Appendix A, "The Significance Determination Process for Findings At-Power,"
issued June 19, 2012, the inspectors screened the finding for safety significance and
determined it to be of very low safety significance (Green), because the finding did not represent an actual loss of system or function.  After inspector questioning, Entergy performed an operability evaluation, which provided sufficient bases to conclude the Unit 3 baffle assembly would support ECCS operability.  This finding is related to the cross-cutting
aspect of Problem Identification and Resolution, Operating Experience, because Entergy did
 
not effectively evaluate relevant internal and external operating experience.  Specifically, Entergy did not adequately evaluate the impact of degraded baffle bolts at Unit 3 when relevant operating experience was identified at Unit 2.  [P.5 - Operating Experience] (Section 1R15)
 
4    Green.  The inspectors identified a Green NCV of Technical Specification (TS) 5.4.1, "Procedures," for Entergy's failure to implement procedure OAP-007, "Containment Entry and Egress."  Specifically, workers transiting the inner and outer crane wall sections of
containment failed to maintain at least one (of two) flow channeling gate closed to ensure availability of the containment sumps to provide suction for the ECCS.  Entergy immediately coached the gate monitor and restored the gates to an acceptable position.  Entergy
generated CR-IP2-2016-04036 to address this issue.
 
This performance deficiency is more than minor because it was associated with the
configuration control (shutdown equipment lineup) attribute of the Mitigating Systems cornerstone and affected the cornerstone objective to ensure the availability, reliability, and capability of systems that respond to initiating events to prevent undesirable consequences
(i.e., core damage).  A detailed risk assessment was conducted and determined that the
change in core damage frequency was determined to be 7E-9, therefore, this issue
represents a Green finding.  This finding had a cross-cutting aspect in the area of Human Performance, Avoid Complacency, because Entergy did not consider potential undesired consequences of actions before performing work and implement appropriate error-reduction tools.  Specifically, the work crew did not understand the requirements and potential
consequences prior to commencing work and the gate monitor did not enforce these
requirements to maintain at least one gate locked or pinned closed as required by OAP-007.  [H.12 - Avoid Complacency] (Section 1R20)
Cornerstone:  Barrier Integrity
  Green.  The inspectors identified a Green NCV of 10 CFR 50.65(b)(1) for Entergy's failure to include a function of a safety-related system within the scope of the maintenance rule program.  Specifically, Entergy failed to include the feedwater isolation function performed
by the main boiler feedwater pumps (MBF
Ps) discharge valves, MBFPs, and feedwater regulating valves, which are required to remain functional during and following a design basis event to mitigate the consequence of the accident within the scope of the maintenance
rule monitoring program.  Entergy initiated corrective actions to include the feedwater
isolation function performed by the MBFP discharge valves, MBFPs, and feedwater
regulating valves within the maintenance rule monitoring program.  Entergy entered this issue into the CAP as CR-IP2-2016-03963.
 
This performance deficiency is more than minor because it was associated with barrier
performance attribute of the Barrier Integrity cornerstone and adversely affected the
cornerstone objective to provide reasonable assurance that physical design barriers protect
the public from radionuclide releases caused by accidents or events.  Specifically, the failure to properly scope the feedwater isolation function prevented Entergy from identifying that equipment reliability was no longer effectively controlled through preventive maintenance.  In accordance with IMC 0609.04, "Initial Characterization of Findings," and Exhibit 2 of IMC
0609, Appendix A, "The Significance Determination Process for Findings At-Power," issued
June 19, 2012, the inspectors determined that the finding was of very low safety significance (Green) because the finding did not represent an actual open pathway in the physical integrity of reactor containment, containment isolation system, and heat removal
components.  This finding does not have a cross-cutting aspect since the failure to scope
this equipment into the maintenance rule program was not recognized when Entergy
combined the maintenance rule basis documents for Units 2 and 3 in 2012
and, as a result, is not indicative of current licensee performance.  (Section 4OA3) 
5  REPORT DETAILS
Summary of Plant Status
Unit 2 began the inspection period during RFO 2R22 which lasted 102 days.  Upon completion
of the outage, the operators restarted Unit 2 on June 14, 2016, and increased power slowly to
93 percent for fuel preconditioning.  On June 23, 2016, the operators shutdown the reactor to
repair a service water leak on the 21 component cooling water (CCW) heat exchanger (Hx) inlet
line and replace switchyard breaker 9.  Unit 2 returned to 100 percent power on June 29, 2016.  Unit 2 remained at or near 100 percent power for the remainder of the inspection period. 
Unit 3 began the inspection period at 100 percent power.  On April 26, 2016, a failed controller
caused both heater drain pumps to trip; and the operators reduced power rapidly, stabilizing the
unit at 48 percent power.  Operators returned Unit 3 to 100 percent power on April 27, 2016, and remained at or near 100 percent power for the remainder of the inspection period.
1. REACTOR SAFETY
  Cornerstones:  Initiating Events, Mitigating Systems, and Barrier Integrity
1R04 Equipment Alignment 
Partial System Walkdowns (71111.04Q - 5 samples)
a. Inspection Scope
The inspectors performed partial walkdowns of the following systems:
 
Unit 2  Spent fuel pool cooling system following core offload on May 19, 2016  Shutdown cooling system following core reload on June 6, 2016  CCW system following maintenance on June 28, 2016
Unit 3  32 emergency diesel generator (EDG) following maintenance on May 9, 2016 (this sample was part of an in-depth review of the EDG system)  Residual heat removal pumps following CCW system testing on May 20, 2016
The inspectors selected these systems based on their risk-significance relative to the reactor safety cornerstones at the time they were inspected.  The inspectors reviewed
applicable operating procedures, system diagrams, the updated final safety analysis
report (UFSAR), TSs, work orders (WOs), condition reports (CRs), and the impact of
ongoing work activities on redundant trains of equipment in order to identify conditions that could have impacted system performance of their intended safety functions.  The inspectors also performed field walkdowns of accessible portions of the systems to verify
system components and support equipment were aligned correctly and were operable. 
The inspectors examined the material condition of the components and observed
operating parameters of equipment to verify that there were no deficiencies.  The 
6  inspectors also reviewed whether Entergy had properly identified equipment issues and entered them into the CAP for resolution with the appropriate significance
characterization.  Documents reviewed for each section of this inspection report are listed in the Attachment. 
b. Findings
No findings were identified.
 
1R05 Fire Protection
  Resident Inspector Quarterly Walkdowns (71111.05Q - 6 samples)
a. Inspection Scope
The inspectors conducted tours of the areas listed below to assess the material
condition and operational status of fire protection features.  The inspectors verified that
Entergy controlled combustible materials and ignition sources in accordance with
administrative procedures.  The inspectors verified that fire protection and suppression equipment were available for use as specified in the area pre-fire plan (PFP) and passive fire barriers were maintained in good material condition.  The inspectors also
verified that station personnel implemented compensatory measures for out-of-service
(OOS), degraded, or inoperable fire protection equipment, as applicable, in accordance
with procedures. 
 
Unit 2  Containment, 95-foot elevation, during baffle bolt repair activities with hot work in progress (PFP-203 was reviewed) on June 2, 2016  Residual heat removal pump rooms in primary auxiliary building (PAB), 15-foot elevation (PFP-204 was reviewed), on June 6, 2016  CCW pump room, 68-foot elevation (PFP-209 was reviewed), on June 25, 2016  PAB, 80-foot elevation, CCW heat exchanger area with hot work in progress (PFP-211 was reviewed) on June 25, 2016
Unit 3  32 EDG room, 10-foot elevation (PFP-354 was reviewed), on May 9, 2016  480V switchgear room, 15-foot elevation (PFP-351 was reviewed), on June 30, 2016
b. Findings
No findings were identified.
 
7    1R07 Heat Sink Performance (71111.07A - 1 sample)
a. Inspection Scope
The inspectors reviewed the 32 EDG jacket water and lube oil heat exchanger to
determine its readiness and availability to perform its safety functions.  The inspectors reviewed the design basis for the component and verified Entergy's commitments to
NRC Generic Letter 89-13, "Service Water System Requirements Affecting Safety-Related Equipment."  The inspectors observed the annual cleaning and inspection of the heat exchangers and
reviewed the results of previous inspections of the Unit 3 EDG heat exchangers.  The inspectors discussed the results of the most
recent inspection with engineering staff.  The inspectors verified that Entergy initiated
appropriate corrective actions for identified deficiencies.  The inspectors also verified that the number of tubes plugged within the heat exchanger did not exceed the maximum amount allowed.
 
b. Findings
No findings were identified.
1R08 Inservice Inspection Activities  (71111.08P - 1 sample)
a. Inspection Scope
Inspectors from the NRC Region I Office, specializing in materials and inservice examination activities, observed portions of Entergy's activities involving baffle-former bolt examinations and replacements during Unit 2 RFO 2R22.  The inspectors reviewed
work documentation and examination procedures and results, and discussed these
activities with Entergy.  The inspectors were on-site from April 27 to April 28, 2016, and on May 23, 2016.  The inspectors verified that Entergy completed baffle-former bolt examinations in accordance with their approved procedures which implemented activities described in the Materials Reliability Program (MRP)-227-A, "Pressurized
Water Reactor Internals Inspection and Evaluation Guidelines," as they relate to this
component.  Specifically, the inspectors reviewed the results of the visual and volumetric
examinations of the baffle-former bolts, including capabilities, limitations, and acceptance criteria that were performed during the current RFO.
Non-Destructive Examination Activities
  The inspectors reviewed the ultrasonic testing (UT) procedure used for the examination of the Unit 2 baffle-former bolts to verify the procedure was in accordance with the applicable guidance in MRP-227-A and MRP-228.  The inspectors reviewed the UT data
records and the detailed UT channel analysis for a sample of baffle-former bolts to verify
the examinations and evaluations were performed in accordance with approved
procedures and applicable guidance.  The inspectors reviewed video recordings of the
visual examinations of the baffle-former bolts during the current RFO.  The inspectors also reviewed recorded video of visual examinations performed in 2006 at Unit 2, completed as part of the existing inservice inspection program for the 10-year reactor
vessel examinations, to independently assess the past conditions of the baffle-former
bolts and assembly. 
8  The inspectors reviewed certifications of the UT technicians performing the ultrasonic examinations to verify the examinations were performed by qualified individuals and to verify the results were reviewed and evaluated by certified level III non-destructive examination personnel.
Baffle-Former Bolt Replacement Activities
The inspectors reviewed the baffle-former bolt replacement activities performed as part
of a corrective action to resolve the degraded condition identified at Unit 2.  The inspectors observed a sample of in-process bolt removal activities, which included lock bar milling and bolt hole machining.  The inspectors reviewed the documentation for
in-process and completed bolt installation activities and verified that loose parts
generated as part of the bolt replacements were properly tracked.  The inspectors
verified that bolt replacement activities were performed in accordance with approved procedures.  The inspectors also reviewed the Engineering Change (EC) package associated with the new baffle-former bolt design.  This review is documented in
Section 1R18 of this report.  After completion of the bolt replacement activities, the
inspectors reviewed the video of the final visual examination of the baffle assembly to
verify that the baffle-former bolt work was accomplished as planned and that there were no visual indications of deficiencies.
b. Findings
No findings were identified. 
 
Update to URI 05000247/2016001-01, Baffle-Former Bolts with Identified Anomalies
This inspection was conducted to follow-up on NRC Unresolved Item (URI)
05000247/2016001-01, Baffle-Former Bolts with Identified Anomalies, to determine
whether there was a performance deficiency associated with the degraded baffle-former bolt condition discovered at Unit 2.  The inspectors plan to review additional technical information from Entergy as it becomes available, including any revisions to the root
cause evaluation.  The URI remains open until review of this additional information is
 
completed.  (URI 05000247/2016001-01, Baffle-Former Bolts with Identified
Anomalies)
1R11 Licensed Operator Requalification Program (71111.11Q - 5 samples)
Unit 2 
.1 Quarterly Review of Unit 2 Licensed Operator Requalification Testing and Training
(71111.11Q - 1 sample)
a. Inspection Scope
The inspectors observed Unit 2 licensed operator simulator training on May 24, 2016,
which included reactor coolant pump seal failure with loss of normal heat sink requiring implementation of feed and bleed cooling.  The inspectors evaluated operator performance during the simulated event and verified completion of risk significant
operator actions, including the use of abnormal and emergency operating procedures.
The inspectors assessed the clarity and effectiveness of communications, 
9  implementation of actions in response to alarms and degrading plant conditions, and the oversight and direction provided by the control room supervisor.  The inspectors verified the accuracy and timeliness of the emergency classification made by the shift manager and the TS action statements entered by the shift technical advisor.  Additionally, the inspectors assessed the ability of the crew and training staff to identify and document
 
crew performance problems.
 
b. Findings
  No findings were identified.
.2 Quarterly Review of Unit 3 Licensed Operator Requalification Testing and Training
(71111.11Q - 1 sample)
a. Inspection Scope
The inspectors observed a Unit 3 licensed operator simulator requalification training
evaluated scenario on May 24, 2016, which included failure of a pressurizer pressure
instrument, charging pump trip, loss of 480V safety bus 5A, a small break loss-of-coolant accident (LOCA), and entry into FR-C.2 core cooling.  The inspectors evaluated operator performance during the simulated event and verified completion of risk significant
operator actions, including the use of abnormal and emergency operating procedures.
The inspectors assessed the clarity and effectiveness of communications,
implementation of actions in response to alarms and degrading plant conditions, and the
oversight and direction provided by the control room supervisor.  The inspectors verified the accuracy and timeliness of the emergency classification made by the shift manager and the TS action statements entered by the shift technical advisor.  Additionally, the inspectors assessed the ability of the crew and training staff to identify and document
 
crew performance problems.  b. Findings
  No findings were identified.
 
.3 Quarterly Review of Licensed Operator Performance (71111.11Q - 3 samples)
a. Inspection Scope
The inspectors conducted a focused observation of operator performance in the main
control room.  The inspectors observed pre-job briefings and control room
communications to verify they met the criteria specified in Entergy's administrative procedure EN-OP-115, "Conduct of Operations."  Additionally, the inspectors observed restoration activities to verify that procedure use, crew communications, and
coordination of activities between work groups similarly met established expectations and standards. 
 
   
10  Unit 2  Plant startup from RFO 2R22 on June 16, 2016 including response to a turbine trip without a reactor trip and the subsequent turbine-generator synchronization and transfer of plant electrical loads from offsite power to the unit auxiliary transformer.  Reactor startup and grid synchronization conducted on June 27, 2016. 
Unit 3  Operator response to the feedwater transient which occurred on April 26, 2016
b. Findings
No findings were identified.
1R12 Maintenance Effectiveness (71111.12Q - 4 samples)
.1 Routine Maintenance Effectiveness
a. Inspection Scope
The inspectors reviewed the samples listed below to assess the effectiveness of
maintenance activities on SSCs performance and reliability.  The inspectors reviewed
system health reports, CAP documents, maintenance WOs, and maintenance rule basis


documents to ensure that Entergy was identifying and properly evaluating performance problems within the scope of the maintenance rule. For each SSC sample selected, the inspectors verified that the SSC was properly scoped into the maintenance rule in
                                                                2
accordance with 10 CFR 50.65 and verified that the (a)(2) performance criteria
                                              TABLE OF CONTENTS
established by Entergy was reasonable. As applicable, for SSCs classified as (a)(1), the
SUMMARY .................................................................................................................................... 3
inspectors assessed the adequacy of goals and corrective actions to return these SSCs
REPORT DETAILS ....................................................................................................................... 5
to (a)(2). Additionally, the inspectors ensured that Entergy was identifying and addressing common cause failures that occurred within and across maintenance rule system boundaries.   
1.  REACTOR SAFETY .............................................................................................................. 5
  1R04  Equipment Alignment .................................................................................................. 5
  1R05  Fire Protection ............................................................................................................. 6
  1R07  Heat Sink Performance ............................................................................................... 7
  1R08  Inservice Inspection Activities ..................................................................................... 7
  1R11  Licensed Operator Requalification Program ............................................................... 8
  1R12  Maintenance Effectiveness ....................................................................................... 10
  1R13  Maintenance Risk Assessments and Emergent Work Control .................................. 13
  1R15  Operability Determinations and Functionality Assessments ..................................... 14
  1R18  Plant Modifications .................................................................................................... 19
  1R19  Post-Maintenance Testing ........................................................................................ 20
  1R20  Refueling and Other Outage Activities ...................................................................... 21
  1R22  Surveillance Testing .................................................................................................. 24
  1EP6  Drill Evaluation .......................................................................................................... 25
2.  RADIATION SAFETY .......................................................................................................... 25
  2RS1  Radiological Hazard Assessment and Exposure Controls ........................................ 25
  2RS2  Occupational As Low As Is Reasonably Achievable (ALARA) Planning
          and Controls .............................................................................................................. 26
  2RS7  Radiological Environmental Monitoring Program (REMP) ........................................ 26
4.  OTHER ACTIVITIES ............................................................................................................ 27
  4OA1  Performance Indicator Verification ............................................................................ 27
  4OA2  Problem Identification and Resolution ....................................................................... 28
  4OA3  Follow Up of Events and Notices of Enforcement Discretion .................................... 34
  4OA5  Other Activities .......................................................................................................... 37
  4OA6   Meetings, Including Exit ............................................................................................ 39
SUPPLEMENTARY INFORMATION ........................................................................................ A-1
KEY POINTS OF CONTACT .................................................................................................... A-1
LIST OF ITEMS OPENED, CLOSED, DISCUSSED, AND UPDATED ..................................... A-2
LIST OF DOCUMENTS REVIEWED ........................................................................................ A-3
LIST OF ACRONYMS ............................................................................................................. A-12


  Unit 2 EDGs  Unit 3 EDGs (this sample was part of an in-depth review of the EDG system) Units 2 and 3 CVCS
                                                    3
b. Findings
                                              SUMMARY
Inspection Report 05000247/2016002 and 05000286/2016002; 04/01/2016 - 06/30/2016; Indian
No findings were identified.  
Point Nuclear Generating (Indian Point), Units 2 and 3; Operability Determinations and
Functionality Assessments, Refueling and Other Outage Activities, and Follow Up of Events and
Notices of Enforcement Discretion.
This report covered a three-month period of inspection by resident inspectors and announced
inspections performed by regional inspectors. The inspectors identified three findings of very
low safety significance (Green), which were non-cited violations (NCVs). The significance of
most findings is indicated by their color (i.e., greater than Green, or Green, White, Yellow, Red)
and determined using Inspection Manual Chapter (IMC) 0609, Significance Determination
Process, dated April 29, 2015. Cross-cutting aspects are determined using IMC 0310,
Aspects within the Cross-Cutting Areas, dated December 4, 2014. All violations of
U.S. Nuclear Regulatory Commission (NRC) requirements are dispositioned in accordance with
the NRCs Enforcement Policy, dated February 4, 2015. The NRCs program for overseeing the
safe operation of commercial nuclear power reactors is described in NUREG-1649, Reactor
Oversight Process, Revision 6.
Cornerstone: Mitigating Systems
  Green. The inspectors identified a Green NCV of 10 CFR 50, Appendix B, Criterion V,
    "Instructions, Procedures, and Drawings," because Entergy did not adequately accomplish
    the actions prescribed by procedure EN-OP-104, Operability Determination Process, for a
    degraded condition associated with the Unit 3 baffle-former bolts. Specifically, Entergy
    incorrectly concluded that no degraded or non-conforming condition existed related to the
    Unit 3 baffle-former bolts and exited the operability determination procedure. Entergy
    subsequently performed the remaining steps in the procedure and provided appropriate
    justification for their plans to examine the baffle-former bolts at the next Unit 3 refueling
    outage (RFO). Entergys immediate corrective actions included entering the issue into its
    corrective action program (CAP) as CR-IP3-2016-01961 and documenting an operability
    evaluation to support the basis for operability of the baffle-former bolts and the emergency
    core cooling system (ECCS).
    This performance deficiency is more than minor because it was associated with the
    equipment performance attribute of the Mitigating Systems cornerstone and affected the
    cornerstone objective to ensure the availability, reliability, and capability of systems that
    respond to initiating events to prevent undesirable consequences (i.e., core damage). In
    accordance with IMC 0609.04, Initial Characterization of Findings, and Exhibit 2 of
    IMC 0609, Appendix A, The Significance Determination Process for Findings At-Power,
    issued June 19, 2012, the inspectors screened the finding for safety significance and
    determined it to be of very low safety significance (Green), because the finding did not
    represent an actual loss of system or function. After inspector questioning, Entergy
    performed an operability evaluation, which provided sufficient bases to conclude the Unit 3
    baffle assembly would support ECCS operability. This finding is related to the cross-cutting
    aspect of Problem Identification and Resolution, Operating Experience, because Entergy did
    not effectively evaluate relevant internal and external operating experience. Specifically,
    Entergy did not adequately evaluate the impact of degraded baffle bolts at Unit 3 when
    relevant operating experience was identified at Unit 2. [P.5 - Operating Experience]
    (Section 1R15)


  URI Opened, CVCS Goal Monitoring Under the Maintenance Rule
                                                  4
   Introduction
   Green. The inspectors identified a Green NCV of Technical Specification (TS) 5.4.1,
The inspectors identified issues of potential concern with Entergy's application of 10 CFR 50.65(a)(1), "Requirements for Monitoring the Effectiveness of Maintenance at Nuclear Plants," (the maintenance rule) in regards to the reliability of the Unit 2 CVCS
  Procedures, for Entergys failure to implement procedure OAP-007, Containment Entry
system. These concerns included the establishment of appropriate (a)(1) goals and
  and Egress. Specifically, workers transiting the inner and outer crane wall sections of
11  whether appropriate justification was established that the corrective actions to address identified maintenance weaknesses were effective prior to removal from (a)(1) status. 
  containment failed to maintain at least one (of two) flow channeling gate closed to ensure
Specifically, Entergy may have established restrictive goals without defensible justification and may not have demonstrated their chosen goal before ending the goal
  availability of the containment sumps to provide suction for the ECCS. Entergy immediately
monitoring interval.  
  coached the gate monitor and restored the gates to an acceptable position. Entergy
  generated CR-IP2-2016-04036 to address this issue.
  This performance deficiency is more than minor because it was associated with the
  configuration control (shutdown equipment lineup) attribute of the Mitigating Systems
  cornerstone and affected the cornerstone objective to ensure the availability, reliability, and
  capability of systems that respond to initiating events to prevent undesirable consequences
  (i.e., core damage). A detailed risk assessment was conducted and determined that the
  change in core damage frequency was determined to be 7E-9, therefore, this issue
  represents a Green finding. This finding had a cross-cutting aspect in the area of Human
  Performance, Avoid Complacency, because Entergy did not consider potential undesired
  consequences of actions before performing work and implement appropriate error-reduction
  tools. Specifically, the work crew did not understand the requirements and potential
  consequences prior to commencing work and the gate monitor did not enforce these
  requirements to maintain at least one gate locked or pinned closed as required by OAP-007.
  [H.12 - Avoid Complacency] (Section 1R20)
Cornerstone: Barrier Integrity
  Green. The inspectors identified a Green NCV of 10 CFR 50.65(b)(1) for Entergys failure to
  include a function of a safety-related system within the scope of the maintenance rule
  program. Specifically, Entergy failed to include the feedwater isolation function performed
  by the main boiler feedwater pumps (MBFPs) discharge valves, MBFPs, and feedwater
  regulating valves, which are required to remain functional during and following a design
  basis event to mitigate the consequence of the accident within the scope of the maintenance
  rule monitoring program. Entergy initiated corrective actions to include the feedwater
  isolation function performed by the MBFP discharge valves, MBFPs, and feedwater
  regulating valves within the maintenance rule monitoring program. Entergy entered this
  issue into the CAP as CR-IP2-2016-03963.
  This performance deficiency is more than minor because it was associated with barrier
  performance attribute of the Barrier Integrity cornerstone and adversely affected the
  cornerstone objective to provide reasonable assurance that physical design barriers protect
  the public from radionuclide releases caused by accidents or events. Specifically, the failure
  to properly scope the feedwater isolation function prevented Entergy from identifying that
  equipment reliability was no longer effectively controlled through preventive maintenance.
  In accordance with IMC 0609.04, Initial Characterization of Findings, and Exhibit 2 of IMC
  0609, Appendix A, The Significance Determination Process for Findings At-Power, issued
  June 19, 2012, the inspectors determined that the finding was of very low safety significance
  (Green) because the finding did not represent an actual open pathway in the physical
  integrity of reactor containment, containment isolation system, and heat removal
  components. This finding does not have a cross-cutting aspect since the failure to scope
  this equipment into the maintenance rule program was not recognized when Entergy
  combined the maintenance rule basis documents for Units 2 and 3 in 2012 and, as a result,
  is not indicative of current licensee performance. (Section 4OA3)


                                                5
Description
                                      REPORT DETAILS
Summary of Plant Status
The maintenance rule requires that licensees shall monitor the performance or condition
Unit 2 began the inspection period during RFO 2R22 which lasted 102 days. Upon completion
of structures, systems, or components, against licensee-established goals, in a manner sufficient to provide reasonable assurance that these structures, systems, and  
of the outage, the operators restarted Unit 2 on June 14, 2016, and increased power slowly to
components are capable of fulfilling their intended functions. These goals shall be
93 percent for fuel preconditioning. On June 23, 2016, the operators shutdown the reactor to
established commensurate with safety and, where practical, take into account
repair a service water leak on the 21 component cooling water (CCW) heat exchanger (Hx) inlet
industrywide operating experience. When the performance or condition of a structure, system, or component does not meet established goals, appropriate corrective action shall be taken.  EN-DC-206, "Maintenance Rule (a)(1) Process," provides the  
line and replace switchyard breaker 9. Unit 2 returned to 100 percent power on June 29, 2016.
requirements and processes for managing SSCs for which (a)(2) monitoring has not
Unit 2 remained at or near 100 percent power for the remainder of the inspection period.
demonstrated effective maintenance.  EN-DC-206 specifies that (a)(1) action plans
Unit 3 began the inspection period at 100 percent power. On April 26, 2016, a failed controller
should not be closed until effectiveness of all corrective actions has been demonstrated by meeting performance goals through the monitoring period (or by other means specified in the action plan).  
caused both heater drain pumps to trip; and the operators reduced power rapidly, stabilizing the
unit at 48 percent power. Operators returned Unit 3 to 100 percent power on April 27, 2016,
and remained at or near 100 percent power for the remainder of the inspection period.
1.     REACTOR SAFETY
        Cornerstones: Initiating Events, Mitigating Systems, and Barrier Integrity
1R04 Equipment Alignment
        Partial System Walkdowns (71111.04Q - 5 samples)
    a. Inspection Scope
        The inspectors performed partial walkdowns of the following systems:
        Unit 2
          Spent fuel pool cooling system following core offload on May 19, 2016
          Shutdown cooling system following core reload on June 6, 2016
          CCW system following maintenance on June 28, 2016
        Unit 3
          32 emergency diesel generator (EDG) following maintenance on May 9, 2016 (this
            sample was part of an in-depth review of the EDG system)
          Residual heat removal pumps following CCW system testing on May 20, 2016
        The inspectors selected these systems based on their risk-significance relative to the
        reactor safety cornerstones at the time they were inspected. The inspectors reviewed
        applicable operating procedures, system diagrams, the updated final safety analysis
        report (UFSAR), TSs, work orders (WOs), condition reports (CRs), and the impact of
        ongoing work activities on redundant trains of equipment in order to identify conditions
        that could have impacted system performance of their intended safety functions. The
        inspectors also performed field walkdowns of accessible portions of the systems to verify
        system components and support equipment were aligned correctly and were operable.
        The inspectors examined the material condition of the components and observed
        operating parameters of equipment to verify that there were no deficiencies. The


                                                6
Since 2013, there have been several repeat functional failures of equipment in the  
      inspectors also reviewed whether Entergy had properly identified equipment issues and
CVCS resulting in a failure to meet the performance criterion for reliability. These
      entered them into the CAP for resolution with the appropriate significance
failures included:
      characterization. Documents reviewed for each section of this inspection report are
  A failure of the 23 charging pump on August 6, 2013, after the internal oil pump discharge tubing broke causing the pump to trip on low oil pressure and a loss of charging. The 21 charging pump had tripped for the same reason in 2010.  A failure of the 22 charging pump on January 14, 2014, due to cracked internal check valves caused by an inadequate fill-and-vent that left air in the pump following maintenance. The 21 charging pump had failed due to the same cause in 2013.  A failure of the Unit 2 valve FCV-110A, boric acid flow control valve, to fully open on January 5, 2015.  The valve had insufficient insulation; and as a result, boron crystalized above the valve plug and blocked its movement. The Unit 3 FCV-110A
      listed in the Attachment.
had failed in the same way in 2011, with earlier failures of other valves for the same cause going back to 1997.
  b. Findings
      No findings were identified.
In each case, the CVCS for Unit 2 was already (a)(1), so Entergy either updated the
1R05 Fire Protection
existing (a)(1) action plan or created another one to operate in parallel with the existing
      Resident Inspector Quarterly Walkdowns (71111.05Q - 6 samples)
one.  Upon reviewing the associated (a)(1) action plans, the inspectors noted that in each example Entergy's goals may not have been in accordance with EN-DC-206(a)(1) Process.  It specifies that monitoring intervals should be at least six months for normally
  a. Inspection Scope
operating SSCs, at least three surveillances for SSCs monitored by surveillance and long enough to detect recurrence of the applicable failure mechanism. It also states that
      The inspectors conducted tours of the areas listed below to assess the material
performance goals that provide reasonable assurance that the SSC is capable of
      condition and operational status of fire protection features. The inspectors verified that
performing its intended functions should be monitored throughout the time the SSC is classified (a)(1). EN-DC-206 defines an SSC as any discreet component grouping that has caused a monitoring failure, including any applicable extent of condition.  In the
      Entergy controlled combustible materials and ignition sources in accordance with
      administrative procedures. The inspectors verified that fire protection and suppression
      equipment were available for use as specified in the area pre-fire plan (PFP) and
      passive fire barriers were maintained in good material condition. The inspectors also
      verified that station personnel implemented compensatory measures for out-of-service
      (OOS), degraded, or inoperable fire protection equipment, as applicable, in accordance
      with procedures.
      Unit 2
          Containment, 95-foot elevation, during baffle bolt repair activities with hot work in
          progress (PFP-203 was reviewed) on June 2, 2016
          Residual heat removal pump rooms in primary auxiliary building (PAB), 15-foot
          elevation (PFP-204 was reviewed), on June 6, 2016
          CCW pump room, 68-foot elevation (PFP-209 was reviewed), on June 25, 2016
          PAB, 80-foot elevation, CCW heat exchanger area with hot work in progress
          (PFP-211 was reviewed) on June 25, 2016
      Unit 3
          32 EDG room, 10-foot elevation (PFP-354 was reviewed), on May 9, 2016
          480V switchgear room, 15-foot elevation (PFP-351 was reviewed), on June 30, 2016
  b. Findings
      No findings were identified.


examples provided, NRC inspectors challenged whether Entergy either chose a shorter 
                                                  7
12  monitoring interval or a goal that did not include the applicable extent of condition. Specifically:
1R07 Heat Sink Performance (71111.07A - 1 sample)
  a. Inspection Scope
      The inspectors reviewed the 32 EDG jacket water and lube oil heat exchanger to
      determine its readiness and availability to perform its safety functions. The inspectors
      reviewed the design basis for the component and verified Entergys commitments to
      NRC Generic Letter 89-13, Service Water System Requirements Affecting
      Safety-Related Equipment. The inspectors observed the annual cleaning and
      inspection of the heat exchangers and reviewed the results of previous inspections of
      the Unit 3 EDG heat exchangers. The inspectors discussed the results of the most
      recent inspection with engineering staff. The inspectors verified that Entergy initiated
      appropriate corrective actions for identified deficiencies. The inspectors also verified
      that the number of tubes plugged within the heat exchanger did not exceed the
      maximum amount allowed.
  b. Findings
      No findings were identified.
1R08 Inservice Inspection Activities (71111.08P - 1 sample)
  a. Inspection Scope
      Inspectors from the NRC Region I Office, specializing in materials and inservice
      examination activities, observed portions of Entergys activities involving baffle-former
      bolt examinations and replacements during Unit 2 RFO 2R22. The inspectors reviewed
      work documentation and examination procedures and results, and discussed these
      activities with Entergy. The inspectors were on-site from April 27 to April 28, 2016, and
      on May 23, 2016. The inspectors verified that Entergy completed baffle-former bolt
      examinations in accordance with their approved procedures which implemented
      activities described in the Materials Reliability Program (MRP)-227-A, Pressurized
      Water Reactor Internals Inspection and Evaluation Guidelines, as they relate to this
      component. Specifically, the inspectors reviewed the results of the visual and volumetric
      examinations of the baffle-former bolts, including capabilities, limitations, and
      acceptance criteria that were performed during the current RFO.
      Non-Destructive Examination Activities
      The inspectors reviewed the ultrasonic testing (UT) procedure used for the examination
      of the Unit 2 baffle-former bolts to verify the procedure was in accordance with the
      applicable guidance in MRP-227-A and MRP-228. The inspectors reviewed the UT data
      records and the detailed UT channel analysis for a sample of baffle-former bolts to verify
      the examinations and evaluations were performed in accordance with approved
      procedures and applicable guidance. The inspectors reviewed video recordings of the
      visual examinations of the baffle-former bolts during the current RFO. The inspectors
      also reviewed recorded video of visual examinations performed in 2006 at Unit 2,
      completed as part of the existing inservice inspection program for the 10-year reactor
      vessel examinations, to independently assess the past conditions of the baffle-former
      bolts and assembly.


  The (a)(1) action plan for the broken oil tubing had a goal of no noticeable decrease in 23 charging pump's running oil pressure for the next three quarterly surveillances. The chosen monitoring interval met the procedural expectation, but Entergy limited the monitoring to the 23 charging pump without written justification, when the 21
                                                8
charging pump had failed previously for the same reason and the other pumps were  
      The inspectors reviewed certifications of the UT technicians performing the ultrasonic
susceptible to the same failure mechanism.  During the monitoring interval, the 21
      examinations to verify the examinations were performed by qualified individuals and to
charging pump experienced low oil pressure. When Entergy performed repairs on
      verify the results were reviewed and evaluated by certified level III non-destructive
the 21 charging pump for an unrelated issue, they discovered that the oil tubing had failed in the same way the 23 charging pump oil tubing had failed, although it had not
      examination personnel.
yet caused a pump trip. The (a)(1) action plan for the cracked check valves had a goal of no check valve
      Baffle-Former Bolt Replacement Activities
failure for six months for the next charging pump that underwent maintenance. This happened to be the 22 charging pump.  Entergy chose a six-month monitoring
      The inspectors reviewed the baffle-former bolt replacement activities performed as part
      of a corrective action to resolve the degraded condition identified at Unit 2. The
      inspectors observed a sample of in-process bolt removal activities, which included lock
      bar milling and bolt hole machining. The inspectors reviewed the documentation for
      in-process and completed bolt installation activities and verified that loose parts
      generated as part of the bolt replacements were properly tracked. The inspectors
      verified that bolt replacement activities were performed in accordance with approved
      procedures. The inspectors also reviewed the Engineering Change (EC) package
      associated with the new baffle-former bolt design. This review is documented in
      Section 1R18 of this report. After completion of the bolt replacement activities, the
      inspectors reviewed the video of the final visual examination of the baffle assembly to
      verify that the baffle-former bolt work was accomplished as planned and that there were
      no visual indications of deficiencies.
  b. Findings
      No findings were identified.
      Update to URI 05000247/2016001-01, Baffle-Former Bolts with Identified Anomalies
      This inspection was conducted to follow-up on NRC Unresolved Item (URI)
      05000247/2016001-01, Baffle-Former Bolts with Identified Anomalies, to determine
      whether there was a performance deficiency associated with the degraded baffle-former
      bolt condition discovered at Unit 2. The inspectors plan to review additional technical
      information from Entergy as it becomes available, including any revisions to the root
      cause evaluation. The URI remains open until review of this additional information is
      completed. (URI 05000247/2016001-01, Baffle-Former Bolts with Identified
      Anomalies)
1R11 Licensed Operator Requalification Program (71111.11Q - 5 samples)
      Unit 2
.1    Quarterly Review of Unit 2 Licensed Operator Requalification Testing and Training
      (71111.11Q - 1 sample)
  a. Inspection Scope
      The inspectors observed Unit 2 licensed operator simulator training on May 24, 2016,
      which included reactor coolant pump seal failure with loss of normal heat sink requiring
      implementation of feed and bleed cooling. The inspectors evaluated operator
      performance during the simulated event and verified completion of risk significant
      operator actions, including the use of abnormal and emergency operating procedures.
      The inspectors assessed the clarity and effectiveness of communications,


interval, even though only one of the three char
                                                  9
ging pumps is in service at any given time, and the 22 charging pump only ran for four out of the six months it was monitored. Additionally, the action plan did not justify why a single successful fill-and-vent demonstrated adequate corrective actions. On November 19, 2014, during
      implementation of actions in response to alarms and degrading plant conditions, and the
the six month monitoring interval, the 21 charging pump underwent maintenance
      oversight and direction provided by the control room supervisor. The inspectors verified
      the accuracy and timeliness of the emergency classification made by the shift manager
      and the TS action statements entered by the shift technical advisor. Additionally, the
      inspectors assessed the ability of the crew and training staff to identify and document
      crew performance problems.
  b. Findings
      No findings were identified.
.2    Quarterly Review of Unit 3 Licensed Operator Requalification Testing and Training
      (71111.11Q - 1 sample)
  a. Inspection Scope
      The inspectors observed a Unit 3 licensed operator simulator requalification training
      evaluated scenario on May 24, 2016, which included failure of a pressurizer pressure
      instrument, charging pump trip, loss of 480V safety bus 5A, a small break loss-of-coolant
      accident (LOCA), and entry into FR-C.2 core cooling. The inspectors evaluated operator
      performance during the simulated event and verified completion of risk significant
      operator actions, including the use of abnormal and emergency operating procedures.
      The inspectors assessed the clarity and effectiveness of communications,
      implementation of actions in response to alarms and degrading plant conditions, and the
      oversight and direction provided by the control room supervisor. The inspectors verified
      the accuracy and timeliness of the emergency classification made by the shift manager
      and the TS action statements entered by the shift technical advisor. Additionally, the
      inspectors assessed the ability of the crew and training staff to identify and document
      crew performance problems.
  b. Findings
      No findings were identified.
.3    Quarterly Review of Licensed Operator Performance (71111.11Q - 3 samples)
  a. Inspection Scope
      The inspectors conducted a focused observation of operator performance in the main
      control room. The inspectors observed pre-job briefings and control room
      communications to verify they met the criteria specified in Entergys administrative
      procedure EN-OP-115, Conduct of Operations. Additionally, the inspectors observed
      restoration activities to verify that procedure use, crew communications, and
      coordination of activities between work groups similarly met established expectations
      and standards.


requiring a fill-and-vent, and experienced check valve failure two weeks later on December 4. Entergy documented this as a maintenance rule functional failure, and discussed the possibility that it could be due to an inadequate fill-and-vent, but did not change the (a)(1) action plan. The (a)(1) action plan for FCV-110A specified a monitoring interval of six months to include the winter because the previous valve failures had all occurred during the winter months.  However, the actual monitoring interval documented in the corrective  
                                                10
action was from April to October 2015, and therefore did not cover the winter months
      Unit 2
as intended. In January 2016, Entergy performed maintenance on valve CH-297 on
        Plant startup from RFO 2R22 on June 16, 2016 including response to a turbine trip
Unit 3, which is a heat-traced boric acid valve, and did not properly restore the insulation. The valve function was not impacted because it does not often contain high concentrations of boric acid.  
          without a reactor trip and the subsequent turbine-generator synchronization and
          transfer of plant electrical loads from offsite power to the unit auxiliary transformer.
The (a)(1) action plans described above were all reviewed and approved by the  
        Reactor startup and grid synchronization conducted on June 27, 2016.
maintenance rule expert panel. 
      Unit 3
Further information regarding the performance of these SSCs is required to determine
        Operator response to the feedwater transient which occurred on April 26, 2016
whether these issues of concern represent performance deficiencies and whether they
  b. Findings
      No findings were identified.
1R12 Maintenance Effectiveness (71111.12Q - 4 samples)
.1    Routine Maintenance Effectiveness
  a. Inspection Scope
      The inspectors reviewed the samples listed below to assess the effectiveness of
      maintenance activities on SSCs performance and reliability. The inspectors reviewed
      system health reports, CAP documents, maintenance WOs, and maintenance rule basis
      documents to ensure that Entergy was identifying and properly evaluating performance
      problems within the scope of the maintenance rule. For each SSC sample selected, the
      inspectors verified that the SSC was properly scoped into the maintenance rule in
      accordance with 10 CFR 50.65 and verified that the (a)(2) performance criteria
      established by Entergy was reasonable. As applicable, for SSCs classified as (a)(1), the
      inspectors assessed the adequacy of goals and corrective actions to return these SSCs
      to (a)(2). Additionally, the inspectors ensured that Entergy was identifying and
      addressing common cause failures that occurred within and across maintenance rule
      system boundaries.
        Unit 2 EDGs
        Unit 3 EDGs (this sample was part of an in-depth review of the EDG system)
        Units 2 and 3 CVCS
  b. Findings
      No findings were identified.
      URI Opened, CVCS Goal Monitoring Under the Maintenance Rule
      Introduction
      The inspectors identified issues of potential concern with Entergys application of
      10 CFR 50.65(a)(1), Requirements for Monitoring the Effectiveness of Maintenance at
      Nuclear Plants, (the maintenance rule) in regards to the reliability of the Unit 2 CVCS
      system. These concerns included the establishment of appropriate (a)(1) goals and


are more than minor. (URI 05000247/2016002-01, CVCS Goal Monitoring Under the  
                                        11
Maintenance Rule)
whether appropriate justification was established that the corrective actions to address
  .2 Quality Control
identified maintenance weaknesses were effective prior to removal from (a)(1) status.
a. Inspection Scope
Specifically, Entergy may have established restrictive goals without defensible
The inspectors reviewed the weld repair performed on the 21 CCW heat exchanger service water inlet nozzle for Unit 2 to verify Entergy was properly applying quality controls specified in their quality assurance program. The inspectors reviewed
justification and may not have demonstrated their chosen goal before ending the goal
CAP documents, maintenance WOs, ECs, and engineering procedures
monitoring interval.
associated with the weld repair.  The inspectors verified Entergy specified quality control hold points in
Description
13  accordance with their procedures, properly controlled the quality of materials used during the repair, and adequately justified deviations from the existing design.
The maintenance rule requires that licensees shall monitor the performance or condition
Additionally, the inspectors reviewed the welding procedure specification qualification by the vendor to ensure it was in accordance with American Society of Mechanical
of structures, systems, or components, against licensee-established goals, in a manner
Engineers code.
sufficient to provide reasonable assurance that these structures, systems, and
b. Findings
components are capable of fulfilling their intended functions. These goals shall be
established commensurate with safety and, where practical, take into account
No findings were identified.  
industrywide operating experience. When the performance or condition of a structure,
1R13 Maintenance Risk Assessments and Emergent Work Control (71111.13 - 7 samples)
system, or component does not meet established goals, appropriate corrective action
a. Inspection Scope
shall be taken. EN-DC-206, Maintenance Rule (a)(1) Process, provides the
The inspectors reviewed station evaluation and management of plant risk for the maintenance and emergent work activities listed
requirements and processes for managing SSCs for which (a)(2) monitoring has not
below to verify that Entergy performed the appropriate risk assessments prior to removing equipment for work.  The inspectors
demonstrated effective maintenance. EN-DC-206 specifies that (a)(1) action plans
selected these activities based on potential risk significance relative to the reactor safety
should not be closed until effectiveness of all corrective actions has been demonstrated
cornerstones. As applicable for each activity, the inspectors verified that Entergy performed risk assessments as required by 10 CFR 50.65(a)(4) and that the assessments were accurate and complete.  When Entergy performed emergent work,
by meeting performance goals through the monitoring period (or by other means
the inspectors verified that operations personnel promptly assessed and managed plant
specified in the action plan).
risk.  The inspectors reviewed the scope of maintenance work and discussed the results
Since 2013, there have been several repeat functional failures of equipment in the
of the assessment with the station's probabilistic risk analyst to verify plant conditions
CVCS resulting in a failure to meet the performance criterion for reliability. These
were consistent with the risk assessment. The inspectors also reviewed the TS requirements and inspected portions of redundant safety systems, when applicable, to verify risk analysis assumptions were valid and applicable requirements were met.
failures included:
    A failure of the 23 charging pump on August 6, 2013, after the internal oil pump
    discharge tubing broke causing the pump to trip on low oil pressure and a loss of
    charging. The 21 charging pump had tripped for the same reason in 2010.
    A failure of the 22 charging pump on January 14, 2014, due to cracked internal
    check valves caused by an inadequate fill-and-vent that left air in the pump following
    maintenance. The 21 charging pump had failed due to the same cause in 2013.
    A failure of the Unit 2 valve FCV-110A, boric acid flow control valve, to fully open on
    January 5, 2015. The valve had insufficient insulation; and as a result, boron
    crystalized above the valve plug and blocked its movement. The Unit 3 FCV-110A
    had failed in the same way in 2011, with earlier failures of other valves for the same
    cause going back to 1997.
In each case, the CVCS for Unit 2 was already (a)(1), so Entergy either updated the
existing (a)(1) action plan or created another one to operate in parallel with the existing
one. Upon reviewing the associated (a)(1) action plans, the inspectors noted that in
each example Entergys goals may not have been in accordance with EN-DC-206(a)(1)
Process. It specifies that monitoring intervals should be at least six months for normally
operating SSCs, at least three surveillances for SSCs monitored by surveillance and
long enough to detect recurrence of the applicable failure mechanism. It also states that
performance goals that provide reasonable assurance that the SSC is capable of
performing its intended functions should be monitored throughout the time the SSC is
classified (a)(1). EN-DC-206 defines an SSC as any discreet component grouping that
has caused a monitoring failure, including any applicable extent of condition. In the
examples provided, NRC inspectors challenged whether Entergy either chose a shorter


                                                12
Unit 2  Temporary loss of spent fuel pool cooling due to 345-kilovolt disturbance on April 3, 2016  Equipment hatch closure plug seal demonstration for outage risk on April 5, 2016  Reduced inventory operations during vessel reassembly on June 7, 2016  21 CCW heat exchanger OOS during mode 4 on June 25, 2016
      monitoring interval or a goal that did not include the applicable extent of condition.
Unit 3  32 EDG OOS while Bus Tie BT 4-5 was OOS on May 4, 2016 (this sample was part of an in-depth review of the EDG system)   33 EDG OOS while Bus Tie BT 4-5 was OOS on June 2, 2016  31 EDG OOS while Bus Tie BT 4-5 was OOS on June 21, 2016
      Specifically:
b. Findings
        The (a)(1) action plan for the broken oil tubing had a goal of no noticeable decrease
No findings were identified.  
          in 23 charging pumps running oil pressure for the next three quarterly surveillances.
          The chosen monitoring interval met the procedural expectation, but Entergy limited
          the monitoring to the 23 charging pump without written justification, when the 21
          charging pump had failed previously for the same reason and the other pumps were
          susceptible to the same failure mechanism. During the monitoring interval, the 21
          charging pump experienced low oil pressure. When Entergy performed repairs on
          the 21 charging pump for an unrelated issue, they discovered that the oil tubing had
          failed in the same way the 23 charging pump oil tubing had failed, although it had not
          yet caused a pump trip.
        The (a)(1) action plan for the cracked check valves had a goal of no check valve
          failure for six months for the next charging pump that underwent maintenance. This
          happened to be the 22 charging pump. Entergy chose a six-month monitoring
          interval, even though only one of the three charging pumps is in service at any given
          time, and the 22 charging pump only ran for four out of the six months it was
          monitored. Additionally, the action plan did not justify why a single successful fill-
          and-vent demonstrated adequate corrective actions. On November 19, 2014, during
          the six month monitoring interval, the 21 charging pump underwent maintenance
          requiring a fill-and-vent, and experienced check valve failure two weeks later on
          December 4. Entergy documented this as a maintenance rule functional failure, and
          discussed the possibility that it could be due to an inadequate fill-and-vent, but did
          not change the (a)(1) action plan.
        The (a)(1) action plan for FCV-110A specified a monitoring interval of six months to
          include the winter because the previous valve failures had all occurred during the
          winter months. However, the actual monitoring interval documented in the corrective
          action was from April to October 2015, and therefore did not cover the winter months
          as intended. In January 2016, Entergy performed maintenance on valve CH-297 on
          Unit 3, which is a heat-traced boric acid valve, and did not properly restore the
          insulation. The valve function was not impacted because it does not often contain
          high concentrations of boric acid.
      The (a)(1) action plans described above were all reviewed and approved by the
      maintenance rule expert panel.
      Further information regarding the performance of these SSCs is required to determine
      whether these issues of concern represent performance deficiencies and whether they
      are more than minor. (URI 05000247/2016002-01, CVCS Goal Monitoring Under the
      Maintenance Rule)
.2    Quality Control
  a. Inspection Scope
      The inspectors reviewed the weld repair performed on the 21 CCW heat exchanger
      service water inlet nozzle for Unit 2 to verify Entergy was properly applying quality
      controls specified in their quality assurance program. The inspectors reviewed CAP
      documents, maintenance WOs, ECs, and engineering procedures associated with the
      weld repair. The inspectors verified Entergy specified quality control hold points in


   
                                              13
14  1R15 Operability Determinations and Functionality Assessments (71111.15 - 7 samples)  
      accordance with their procedures, properly controlled the quality of materials used
a. Inspection Scope  
      during the repair, and adequately justified deviations from the existing design.
The inspectors reviewed operability determinations for the following degraded or
      Additionally, the inspectors reviewed the welding procedure specification qualification by
non-conforming conditions:
      the vendor to ensure it was in accordance with American Society of Mechanical
      Engineers code.
  b. Findings
      No findings were identified.
1R13 Maintenance Risk Assessments and Emergent Work Control (71111.13 - 7 samples)
  a. Inspection Scope
      The inspectors reviewed station evaluation and management of plant risk for the
      maintenance and emergent work activities listed below to verify that Entergy performed
      the appropriate risk assessments prior to removing equipment for work. The inspectors
      selected these activities based on potential risk significance relative to the reactor safety
      cornerstones. As applicable for each activity, the inspectors verified that Entergy
      performed risk assessments as required by 10 CFR 50.65(a)(4) and that the
      assessments were accurate and complete. When Entergy performed emergent work,
      the inspectors verified that operations personnel promptly assessed and managed plant
      risk. The inspectors reviewed the scope of maintenance work and discussed the results
      of the assessment with the stations probabilistic risk analyst to verify plant conditions
      were consistent with the risk assessment. The inspectors also reviewed the TS
      requirements and inspected portions of redundant safety systems, when applicable, to
      verify risk analysis assumptions were valid and applicable requirements were met.
      Unit 2
        Temporary loss of spent fuel pool cooling due to 345-kilovolt disturbance on
          April 3, 2016
        Equipment hatch closure plug seal demonstration for outage risk on April 5, 2016
        Reduced inventory operations during vessel reassembly on June 7, 2016
        21 CCW heat exchanger OOS during mode 4 on June 25, 2016
      Unit 3
        32 EDG OOS while Bus Tie BT 4-5 was OOS on May 4, 2016 (this sample was part
          of an in-depth review of the EDG system)
        33 EDG OOS while Bus Tie BT 4-5 was OOS on June 2, 2016
        31 EDG OOS while Bus Tie BT 4-5 was OOS on June 21, 2016
  b. Findings
      No findings were identified.


                                                14
Unit 2   23 EDG failure to run on March 7, 2016, and subsequent failure to pass the surveillance test on March 10, 2016, as identified in CR-IP2-2016-01260 Operability determination for N33 gamma metrics wide range nuclear instrument channel in CR-IP2-2016-03660 on June 13, 2016 Pressurizer level transmitter LT-461 reads high in CR-IP-2016-3806 on June 14, 2016 Through-wall leak in line 411, service water inlet to the 21 CCW heat exchanger, on June 15, 2016  
1R15 Operability Determinations and Functionality Assessments (71111.15 - 7 samples)
  a. Inspection Scope
Unit 3   Immediate operability determination of the degraded condition of the baffle-former bolts identified from Unit 2 operating experience in CR-IP3-2016-01035 on April 1, 2016 Anomalies noted during digital metal impact monitoring system self-test in CR-IP3-2015-03468 on April 1, 2016 Prompt operability determination of the degraded condition of the baffle-former bolts identified from Unit 2 operating experience in CR-IP2-2016-03660 on June 30, 2016  
      The inspectors reviewed operability determinations for the following degraded or
The inspectors selected these issues based on the risk significance of the associated  
      non-conforming conditions:
components and systems. The inspectors evaluated the technical adequacy of the  
      Unit 2
operability determinations to assess whether TS operability was properly justified and  
        23 EDG failure to run on March 7, 2016, and subsequent failure to pass the
the subject component or system remained available such that no unrecognized  
          surveillance test on March 10, 2016, as identified in CR-IP2-2016-01260
increase in risk occurred. The inspectors compared the operability and design criteria in the appropriate sections of the TSs and UFSAR to Entergy's evaluations to determine whether the components or systems were operable.  
        Operability determination for N33 gamma metrics wide range nuclear instrument
          channel in CR-IP2-2016-03660 on June 13, 2016
        Pressurizer level transmitter LT-461 reads high in CR-IP-2016-3806 on June 14,
          2016
        Through-wall leak in line 411, service water inlet to the 21 CCW heat exchanger, on
          June 15, 2016
      Unit 3
        Immediate operability determination of the degraded condition of the baffle-former
          bolts identified from Unit 2 operating experience in CR-IP3-2016-01035 on April 1,
          2016
        Anomalies noted during digital metal impact monitoring system self-test in
          CR-IP3-2015-03468 on April 1, 2016
        Prompt operability determination of the degraded condition of the baffle-former bolts
          identified from Unit 2 operating experience in CR-IP2-2016-03660 on June 30, 2016
      The inspectors selected these issues based on the risk significance of the associated
      components and systems. The inspectors evaluated the technical adequacy of the
      operability determinations to assess whether TS operability was properly justified and
      the subject component or system remained available such that no unrecognized
      increase in risk occurred. The inspectors compared the operability and design criteria in
      the appropriate sections of the TSs and UFSAR to Entergys evaluations to determine
      whether the components or systems were operable.
      The inspectors confirmed, where appropriate, compliance with bounding limitations
      associated with the evaluations. Where compensatory measures were required to
      maintain operability, the inspectors determined whether the measures in place would
      function as intended and were properly controlled by Entergy. The inspectors
      determined, where appropriate, compliance with bounding limitations associated with the
      evaluations.
  b. Findings
      Introduction. The inspectors identified a Green NCV of 10 CFR 50, Appendix B,
      Criterion V, "Instructions, Procedures, and Drawings," because Entergy did not
      adequately accomplish the actions prescribed by procedure EN-OP-104 for a degraded
      condition associated with the Unit 3 baffle-former bolts. Specifically, Entergy incorrectly
      concluded that no degraded or non-conforming condition existed related to the Unit 3


                                          15
The inspectors confirmed, where appropriate, compliance with bounding limitations
baffle-former bolts and exited the operability determination procedure. Entergy
associated with the evaluations.  Where compensatory measures were required to maintain operability, the inspectors determined whether the measures in place would function as intended and were properly controlled by Entergy.  The inspectors
subsequently performed the remaining steps in the procedure and provided appropriate
determined, where appropriate, compliance with bounding limitations associated with the
justification for their plans to examine the baffle-former bolts at the next Unit 3 RFO.
evaluations.
Description. On March 29, 2016, Entergy identified baffle-former (baffle) bolt
b. Findings
degradation at Indian Point Unit 2 that was determined to be unanalyzed because it did
not meet the minimum acceptable bolt pattern analysis developed to support plant
Introduction.  The inspectors identified a Green NCV of 10 CFR 50, Appendix B, Criterion V, "Instructions, Procedures, and Drawings," because Entergy did not
startup. Entergy staff identified a total of 227 baffle bolts out of a population of 832 that
adequately accomplish the actions prescribed by procedure EN-OP-104 for a degraded
were potentially degraded (182 bolts had UT indications; 31 had visual indications of
condition associated with the Unit 3 baffle-former bolts.  Specifically, Entergy incorrectly concluded that no degraded or non-conforming condition existed related to the Unit 3 
failure; and 14 were inaccessible for testing and conservatively assumed to be
15  baffle-former bolts and exited the operability determination procedure. Entergy subsequently performed the remaining steps in the procedure and provided appropriate  
degraded). Entergy staff entered this problem into the CAP as CR-IP2-2016-02081,
justification for their plans to examine the baffle-former bolts at the next Unit 3 RFO.  
performed a root cause evaluation, and replaced the degraded bolts on Unit 2. Due to
Description. On March 29, 2016, Entergy identified baffle-former ("baffle") bolt degradation at Indian Point Unit 2 that was determined to be unanalyzed because it did  
not meet the minimum acceptable bolt pattern analysis developed to support plant  
startup. Entergy staff identified a total of 227 baffle bolts out of a population of 832 that  
were potentially degraded (182 bolts had UT indications; 31 had visual indications of failure; and 14 were inaccessible for testing and conservatively assumed to be degraded). Entergy staff entered this problem into the CAP as CR-IP2-2016-02081,  
performed a root cause evaluation, and replaced the degraded bolts on Unit 2. Due to  
the number of baffle bolt indications discovered on Unit 2, Entergy staff initiated CR-IP3-
the number of baffle bolt indications discovered on Unit 2, Entergy staff initiated CR-IP3-
2016-01035 on April 21, 2016, and performed an immediate operability determination (IOD) in accordance with Entergy procedure EN-OP-104 Section 5.3, to evaluate the baffle bolts and baffle-former assembly structure on Unit 3. Entergy staff planned further  
2016-01035 on April 21, 2016, and performed an immediate operability determination
corrective actions to move up the planned Unit 3 baffle bolt ultrasonic examinations to  
(IOD) in accordance with Entergy procedure EN-OP-104 Section 5.3, to evaluate the
the next RFO in spring 2017.  
baffle bolts and baffle-former assembly structure on Unit 3. Entergy staff planned further
 
corrective actions to move up the planned Unit 3 baffle bolt ultrasonic examinations to
The inspectors reviewed the design basis and current licensing basis documents for Indian Point Unit 3 to identify the specific safety functions of the baffle bolts. The baffle  
the next RFO in spring 2017.
bolts are part of the baffle former assembly structure located in the reactor pressure  
The inspectors reviewed the design basis and current licensing basis documents for
vessel. The bolts secure a series of vertical metal plates called baffle plates, which help  
Indian Point Unit 3 to identify the specific safety functions of the baffle bolts. The baffle
direct water up through the nuclear fuel assemblies to ensure proper cooling of the fuel.
bolts are part of the baffle former assembly structure located in the reactor pressure
A sufficient number of baffle bolts are required to secure the plates to ensure proper core flow during normal and postulated accident conditions, and also to ensure that control rods can be inserted to shut down the reactor.  
vessel. The bolts secure a series of vertical metal plates called baffle plates, which help
 
direct water up through the nuclear fuel assemblies to ensure proper cooling of the fuel.
A sufficient number of baffle bolts are required to secure the plates to ensure proper
The inspectors reviewed Entergy's IOD issued on April 21, 2016, and concluded the  
core flow during normal and postulated accident conditions, and also to ensure that
immediate determination was completed in accordance with Section 5.3 of procedure  
control rods can be inserted to shut down the reactor.
EN-OP-104. The IOD provided sufficient technical detail to support the initial conclusion, based on limited information, that the Unit 3 baffle bolts would retain sufficient capability  
The inspectors reviewed Entergys IOD issued on April 21, 2016, and concluded the
to perform their intended functions. Specifically, the IOD stated that Unit 2 baffle bolt  
immediate determination was completed in accordance with Section 5.3 of procedure
failures were likely due to irradiation-assisted stress corrosion cracking (IASCC) and that  
EN-OP-104. The IOD provided sufficient technical detail to support the initial conclusion,
the Unit 3 baffle bolts were also susceptible because they both utilize a baffle bolt design  
based on limited information, that the Unit 3 baffle bolts would retain sufficient capability
with similar geometry and material to other plants with bolt failures. The IOD concluded that Unit 3 baffle bolt degradation would likely not be as significant as Unit 2, and that the Unit 3 baffle former assembly was currently operable pending further evaluation  
to perform their intended functions. Specifically, the IOD stated that Unit 2 baffle bolt
because of the following differences with Unit 2: (1) less effective full power years of  
failures were likely due to irradiation-assisted stress corrosion cracking (IASCC) and that
operation; (2) less neutron fluence levels (i.e., irradiation); (3) less pressure differential  
the Unit 3 baffle bolts were also susceptible because they both utilize a baffle bolt design
across the baffle plates; and (4) less fatigue-induced loading cycles on the bolts over the operating life of the plant. The inspectors concluded that there was no immediate safety  
with similar geometry and material to other plants with bolt failures. The IOD concluded
concern.  
that Unit 3 baffle bolt degradation would likely not be as significant as Unit 2, and that
the Unit 3 baffle former assembly was currently operable pending further evaluation
On May 5, 2016, Entergy staff revised the operability input for CR-IP3-2016-01035 under  
because of the following differences with Unit 2: (1) less effective full power years of
corrective action #2. The inspectors noted that Entergy staff concluded an operability  
operation; (2) less neutron fluence levels (i.e., irradiation); (3) less pressure differential
evaluation was not needed, in part, because "the baffle-former bolts are not required by TS and are not described in the UFSAR.The inspectors noted that while the baffle bolts are not described in these documents, their failure in sufficient numbers could have  
across the baffle plates; and (4) less fatigue-induced loading cycles on the bolts over the
consequential effects on the TS-controlled ECCS if the baffle plates were to become  
operating life of the plant. The inspectors concluded that there was no immediate safety
detached or deformed. This was described in Entergy's bolt pattern analysis report
concern.
16  documenting an acceptable bolt pattern prior to the spring 2016 RFO.  The inspectors reviewed Unit 3 TS 3.5.2, "ECCS - Operating," which requires multiple trains of ECCS to
On May 5, 2016, Entergy staff revised the operability input for CR-IP3-2016-01035 under
be operable.  The inspectors concluded that since the baffle bolts support the ECCS, which is subject to TS, Entergy's decision to not perform further evaluation of the operability determination was inconsistent with EN-OP-104.  Specifically, Section 5.1(7)
corrective action #2. The inspectors noted that Entergy staff concluded an operability
of Entergy's procedure EN-OP-104 requires that an operability determination be
evaluation was not needed, in part, because the baffle-former bolts are not required by
performed whenever a condition exists in the supporting SCC that may affect the ability
TS and are not described in the UFSAR. The inspectors noted that while the baffle
of the TS-controlled SSC to perform its specified safety function.
bolts are not described in these documents, their failure in sufficient numbers could have
 
consequential effects on the TS-controlled ECCS if the baffle plates were to become
Further, the inspectors noted that Entergy staff concluded a degraded condition did not exist in Unit 3, and therefore, an operability evaluation was not required as a follow-up to
detached or deformed. This was described in Entergys bolt pattern analysis report
the immediate determination.  The documented basis provided was the differences
between the two units, plant operating data, and fuel performance.  The inspectors noted
that plant operating data and fuel performance from Unit 2 did not result in identification of the bolt degradation; therefore, the absence of indications for these problems on Unit 3 was technically insufficient to support Entergy's conclusion that there was no degraded
condition on Unit 3.
 
The inspectors' review of procedure EN-OP-104, Section 3.0, identified that examples of the effects of equipment aging and operating experience can be sources of information considered to enter the operability or functionality process.  The inspectors
acknowledged that licensees apply judgment in these decisions.  In this particular
instance, the inspectors considered that operating experience was available that showed
the Unit 3 baffle bolts were subject to IASCC and that plants of similar design (4-loop
Westinghouse pressurized water reactors with a down-flow configuration and baffle bolts of 347 material and similar dimensions) were subject to greater amounts of bolt degradation compared to other reactor designs.  Furthermore, the inspectors noted the
baffle bolts had experienced levels of neutron radiation exposure above the threshold for
IASCC initiation as referenced in NUREG/CR-7027, "Degradation of LWR Core Internal
Materials due to Neutron Irradiation."
Based on the above information available to Entergy staff, the inspectors concluded that
Entergy's basis for determining that a degraded condition did not exist on Unit 3 was not
technically supported.  The inspectors noted that in completing an IOD in EN-OP-104,
Step 5.3.2 states "determine if there is an ongoing degradation mechanism that may
impact future operability based on changing conditions, specifically consider the SSCs specified safety function and mission time."  On May 5, 2016, Entergy's basis for concluding an operability evaluation was not required and exiting the operability
determination procedure at Step 5.3.3 was inconsistent with this procedural requirement
because their IOD concluded Unit 3 was susceptible to baffle bolt degradation, which is
time based and subject to changing conditions including fatigue inducing loading cycles and neutron fluence.  As a result, the inspectors concluded Entergy staff did not complete the additional actions prescribed by EN-OP-104 to perform an operability
evaluation.  Specifically, Step 5.3.9 states in part "if an Operability Evaluation is required
then perform the following:  Proceed to Subsection 5.5, Operability Evaluation."
 
On July 11, 2016, Entergy staff subsequently completed the steps in EN-OP-104 and performed an operability evaluation, which assumed an estimated number of baffle-former bolt failures based on the degradation found in Unit 2, and adjusted to take credit
for the small number of inaccessible bolts and a sample of bolts extracted with high
removal torque that indicated residual structural capacity.  The inspectors determined 
17  this estimated number of bolt failures was conservative because the evaluation did not credit the baffle-edge bolts or the differences in operational history between the two units
such as neutron fluence levels or fatigue from thermal cycles.  The operability evaluation concluded that the Unit 3 baffle bolts would perform as intended to secure the baffle plates from being dislodged.  The inspectors concluded that Entergy's operability
evaluation provided appropriate basis to conclude that the Unit 3 baffle assembly would
support ECCS operability until the planned Unit 3 RFO in spring 2017.
 
Analysis.  The inspectors determined that Entergy's failure to adequately accomplish the actions prescribed in EN-OP-104 for a degraded condition and perform an operability
evaluation associated with the Unit 3 baffle-former bolts was a performance deficiency. 
 
Specifically, Entergy incorrectly concluded that no degraded or non-conforming condition existed related to the Unit 3 baffle-former bolts and exited the operability determination
procedure.  As a result, Entergy's initial documentation did not provide sufficient basis for operability and continued operation until questioned by NRC inspectors.
This finding is more than minor because it is associated with the equipment performance
attribute of the Mitigating Systems cornerstone and affected the cornerstone objective to
ensure the availability, reliability, and capability of systems that respond to initiating events to prevent undesirable consequences (i.e., core damage).  This issue was also similar to example 3.j of IMC 0612, Appendix E, "Examples of Minor Issues," because
the condition resulted in reasonable doubt of operability of the ECCS and additional
analysis was necessary to verify operability.  In accordance with IMC 0609.04, "Initial
Characterization of Findings," and Exhibit 2 of IMC 0609, Appendix A, "The Significance
Determination Process for Findings At-Power," issued June 19, 2012, the inspectors screened the finding for safety significance and determined it to be of very low safety significance (Green), since the finding did not represent an actual loss of system or
function.  After inspector questioning, Entergy performed an operability evaluation, which
provided sufficient bases to conclude the Unit 3 baffle assembly would support ECCS
operability.  This finding is related to the cross-cutting aspect of Problem Identification and Resolution, Operating Experience, because Entergy did not effectively evaluate
relevant internal and external operating ex
perience.  Specifically, Entergy did not adequately evaluate the impact of degraded baffle bolts at Unit 3 when relevant
operating experience was identified at Unit 2. [P.5] 


                                          16
Enforcement. 10 CFR 50, Appendix B, Criterion V, "Instructions, Procedures, and Drawings," states, in part, that activities affecting quality shall be prescribed by
documenting an acceptable bolt pattern prior to the spring 2016 RFO. The inspectors
documented procedures of a type appropriate to the circumstances and shall be  
reviewed Unit 3 TS 3.5.2, ECCS - Operating, which requires multiple trains of ECCS to
accomplished in accordance with those procedures. The introduction to Appendix B
be operable. The inspectors concluded that since the baffle bolts support the ECCS,
states that 'quality assurance' comprises all those planned and systematic actions necessary to provide adequate confidence that a structure, system, or component (SSC) will perform satisfactorily in service.  Procedure EN-OP-104, Step 5.3[2], related to immediate operability, states "Determine if there is an ongoing degradation mechanism  
which is subject to TS, Entergys decision to not perform further evaluation of the
that may impact future operability based on changing conditions, specifically consider  
operability determination was inconsistent with EN-OP-104. Specifically, Section 5.1(7)
the SSCs specified safety function and mission time.Step 5.3(3) follows with, in part "If
of Entergys procedure EN-OP-104 requires that an operability determination be
no Degraded or Non-conforming Condition exists, then perform the following as the
performed whenever a condition exists in the supporting SCC that may affect the ability
Immediate Determination:" "Declare the SSC Operable" and "Exit this procedure."
of the TS-controlled SSC to perform its specified safety function.
Contrary to the above, from May 5, 2016 until July 11, 2016, Entergy did not adequately
Further, the inspectors noted that Entergy staff concluded a degraded condition did not
accomplish actions as prescribed by EN-OP-104 for a degraded condition associated
exist in Unit 3, and therefore, an operability evaluation was not required as a follow-up to
with the Unit 3 baffle-former bolts. Specifically, Entergy incorrectly concluded that no 
the immediate determination. The documented basis provided was the differences
18  degraded or non-conforming condition existed related to the Unit 3 baffle-former bolts and exited the operability determination procedure. The NRC determined this is contrary
between the two units, plant operating data, and fuel performance. The inspectors noted
to EN-OP-104 because a comparison of Unit 2 and 3 operational factors resulted in Entergy concluding that the Unit 3 baffle bolts would likely be affected due to the same degradation mechanism.  Entergy's corrective actions included entering the issue into
that plant operating data and fuel performance from Unit 2 did not result in identification
the CAP and documenting an operability evaluation to support the basis for operability of
of the bolt degradation; therefore, the absence of indications for these problems on Unit
the baffle bolts and ECCS.  Because this issue is of very low safety significance (Green) and Entergy entered this into their CAP as CR-IP3-2016-01961, this finding is being
3 was technically insufficient to support Entergys conclusion that there was no degraded
treated as an NCV consistent with Section 2.3.2.a of the Enforcement Policy.  (NCV 05000286/2016002-02, Failure to Follow Operability Determination Procedure for
condition on Unit 3.
Unit 3 Baffle-Former Bolts)
The inspectors review of procedure EN-OP-104, Section 3.0, identified that examples of
Update to URI 05000247/2016001-06, 23 Emergency Diesel Generator Automatic Voltage Regulator Failure
the effects of equipment aging and operating experience can be sources of information
considered to enter the operability or functionality process. The inspectors
Introduction.  The NRC opened a URI in Inspection Report 05000247/2016001 related to two failures of the 23 EDG to run and maintain bus voltage on March 7, 2016, and to  
acknowledged that licensees apply judgment in these decisions. In this particular
provide adequate control of bus voltage on March 10, 2016.  This report provides an
instance, the inspectors considered that operating experience was available that showed
update of the status of this URI.
the Unit 3 baffle bolts were subject to IASCC and that plants of similar design (4-loop
Description.  On March 7, 2016, approximately one hour after the trip of the 3A normal feed breaker, the 23 EDG tripped on overcurrent while powering the 6A 480V safety bus. 
Westinghouse pressurized water reactors with a down-flow configuration and baffle bolts
The 6A bus remained de-energized for approximately one hour until the crew restored
of 347 material and similar dimensions) were subject to greater amounts of bolt
the 6A bus via off-site power. The 23 EDG was declared inoperable.  All four 480V
degradation compared to other reactor designs. Furthermore, the inspectors noted the
safety buses were restored to off-site power.  Entergy replaced the overcurrent relays and retested the 23 EDG satisfactorily on March 8, 2016.  However, bench testing of the overcurrent relays demonstrated that they were accurately calibrated.   
baffle bolts had experienced levels of neutron radiation exposure above the threshold for
IASCC initiation as referenced in NUREG/CR-7027, Degradation of LWR Core Internal
Materials due to Neutron Irradiation.
Based on the above information available to Entergy staff, the inspectors concluded that
Entergys basis for determining that a degraded condition did not exist on Unit 3 was not
technically supported. The inspectors noted that in completing an IOD in EN-OP-104,
Step 5.3.2 states determine if there is an ongoing degradation mechanism that may
impact future operability based on changing conditions, specifically consider the SSCs
specified safety function and mission time. On May 5, 2016, Entergys basis for
concluding an operability evaluation was not required and exiting the operability
determination procedure at Step 5.3.3 was inconsistent with this procedural requirement
because their IOD concluded Unit 3 was susceptible to baffle bolt degradation, which is
time based and subject to changing conditions including fatigue inducing loading cycles
and neutron fluence. As a result, the inspectors concluded Entergy staff did not
complete the additional actions prescribed by EN-OP-104 to perform an operability
evaluation. Specifically, Step 5.3.9 states in part if an Operability Evaluation is required
then perform the following: Proceed to Subsection 5.5, Operability Evaluation.
On July 11, 2016, Entergy staff subsequently completed the steps in EN-OP-104 and
performed an operability evaluation, which assumed an estimated number of baffle-
former bolt failures based on the degradation found in Unit 2, and adjusted to take credit
for the small number of inaccessible bolts and a sample of bolts extracted with high
removal torque that indicated residual structural capacity. The inspectors determined


                                            17
Subsequently, on March 10, 2016, during performance of PT-R14, "Automatic Safety
this estimated number of bolt failures was conservative because the evaluation did not
Injection System Electrical Load and Blackout Test," the 23 EDG exhibited anomalous behavior during the train 'B' load sequencing. During this test, the voltage on safety bus
credit the baffle-edge bolts or the differences in operational history between the two units
6A dropped to approximately 200V when
such as neutron fluence levels or fatigue from thermal cycles. The operability evaluation
the 23 auxiliary feedwater pump was sequenced onto the bus (CR-IP2-2016-01430) and the sequencer failed to complete the  
concluded that the Unit 3 baffle bolts would perform as intended to secure the baffle
first two sequences. The 23 EDG was again declared inoperable and the period of  
plates from being dislodged. The inspectors concluded that Entergys operability
inoperability was backdated to March 7, 2016, when it originally tripped. Further
evaluation provided appropriate basis to conclude that the Unit 3 baffle assembly would
troubleshooting and additional failure modes analysis by Entergy initially determined that the cause of both events may have been a degraded resistor (R25) on the 23 EDG
support ECCS operability until the planned Unit 3 RFO in spring 2017.
automatic voltage regulator (AVR) card.  
Analysis. The inspectors determined that Entergys failure to adequately accomplish the
actions prescribed in EN-OP-104 for a degraded condition and perform an operability
evaluation associated with the Unit 3 baffle-former bolts was a performance deficiency.
Specifically, Entergy incorrectly concluded that no degraded or non-conforming condition
existed related to the Unit 3 baffle-former bolts and exited the operability determination
procedure. As a result, Entergys initial documentation did not provide sufficient basis
for operability and continued operation until questioned by NRC inspectors.
This finding is more than minor because it is associated with the equipment performance
attribute of the Mitigating Systems cornerstone and affected the cornerstone objective to
ensure the availability, reliability, and capability of systems that respond to initiating
events to prevent undesirable consequences (i.e., core damage). This issue was also
similar to example 3.j of IMC 0612, Appendix E, Examples of Minor Issues, because
the condition resulted in reasonable doubt of operability of the ECCS and additional
analysis was necessary to verify operability. In accordance with IMC 0609.04, Initial
Characterization of Findings, and Exhibit 2 of IMC 0609, Appendix A, The Significance
Determination Process for Findings At-Power, issued June 19, 2012, the inspectors
screened the finding for safety significance and determined it to be of very low safety
significance (Green), since the finding did not represent an actual loss of system or
function. After inspector questioning, Entergy performed an operability evaluation, which
provided sufficient bases to conclude the Unit 3 baffle assembly would support ECCS
operability. This finding is related to the cross-cutting aspect of Problem Identification
and Resolution, Operating Experience, because Entergy did not effectively evaluate
relevant internal and external operating experience. Specifically, Entergy did not
adequately evaluate the impact of degraded baffle bolts at Unit 3 when relevant
operating experience was identified at Unit 2. [P.5]
Enforcement. 10 CFR 50, Appendix B, Criterion V, Instructions, Procedures, and
Drawings, states, in part, that activities affecting quality shall be prescribed by
documented procedures of a type appropriate to the circumstances and shall be
accomplished in accordance with those procedures. The introduction to Appendix B
states that quality assurance comprises all those planned and systematic actions
necessary to provide adequate confidence that a structure, system, or component (SSC)
will perform satisfactorily in service. Procedure EN-OP-104, Step 5.3[2], related to
immediate operability, states Determine if there is an ongoing degradation mechanism
that may impact future operability based on changing conditions, specifically consider
the SSCs specified safety function and mission time. Step 5.3(3) follows with, in part If
no Degraded or Non-conforming Condition exists, then perform the following as the
Immediate Determination: Declare the SSC Operable and Exit this procedure.
Contrary to the above, from May 5, 2016 until July 11, 2016, Entergy did not adequately
accomplish actions as prescribed by EN-OP-104 for a degraded condition associated
with the Unit 3 baffle-former bolts. Specifically, Entergy incorrectly concluded that no


                                          18
The 23 EDG AVR card was replaced, and the 23 EDG was again tested satisfactorily.
degraded or non-conforming condition existed related to the Unit 3 baffle-former bolts
The voltage anomaly issues exhibited during the March 10, 2016, test were documented in CR-IP2-2016-01430 which was closed in CR-IP2-2016-01260 to be included in the causal assessment associated with the tripping of 23 EDG breaker on March 7, 2016.
and exited the operability determination procedure. The NRC determined this is contrary
Entergy assigned a vendor to perform laboratory bench testing and failure analysis of  
to EN-OP-104 because a comparison of Unit 2 and 3 operational factors resulted in
the 23 EDG AVR card. The vendor report attributed the cause of the March 10, 2016,  
Entergy concluding that the Unit 3 baffle bolts would likely be affected due to the same
loss of voltage control to a degraded solder joint on the AVR card. However, the vendor  
degradation mechanism. Entergys corrective actions included entering the issue into
report explicitly did not attribute the event on March 7, 2016, to the same cause. Entergy assigned a corrective action in CR-IP2-2016-01260 to review the cause of the
the CAP and documenting an operability evaluation to support the basis for operability of
 
the baffle bolts and ECCS. Because this issue is of very low safety significance (Green)
19  23 EDG overcurrent trip on March 7, 2016, in light of the vendor report.  The inspectors determined that the issue of concern remains open as a URI until this causal
and Entergy entered this into their CAP as CR-IP3-2016-01961, this finding is being
assessment has been completed by Entergy and assessed by NRC.  (URI 05000247/2016001-06, 23 Emergency Diesel Generator Automatic Voltage
treated as an NCV consistent with Section 2.3.2.a of the Enforcement Policy. (NCV
05000286/2016002-02, Failure to Follow Operability Determination Procedure for
Unit 3 Baffle-Former Bolts)
Update to URI 05000247/2016001-06, 23 Emergency Diesel Generator Automatic
Voltage Regulator Failure
Introduction. The NRC opened a URI in Inspection Report 05000247/2016001 related to
two failures of the 23 EDG to run and maintain bus voltage on March 7, 2016, and to
provide adequate control of bus voltage on March 10, 2016. This report provides an
update of the status of this URI.
Description. On March 7, 2016, approximately one hour after the trip of the 3A normal
feed breaker, the 23 EDG tripped on overcurrent while powering the 6A 480V safety bus.
The 6A bus remained de-energized for approximately one hour until the crew restored
the 6A bus via off-site power. The 23 EDG was declared inoperable. All four 480V
safety buses were restored to off-site power. Entergy replaced the overcurrent relays
and retested the 23 EDG satisfactorily on March 8, 2016. However, bench testing of the
overcurrent relays demonstrated that they were accurately calibrated.
Subsequently, on March 10, 2016, during performance of PT-R14, Automatic Safety
Injection System Electrical Load and Blackout Test, the 23 EDG exhibited anomalous
behavior during the train B load sequencing. During this test, the voltage on safety bus
6A dropped to approximately 200V when the 23 auxiliary feedwater pump was
sequenced onto the bus (CR-IP2-2016-01430) and the sequencer failed to complete the
first two sequences. The 23 EDG was again declared inoperable and the period of
inoperability was backdated to March 7, 2016, when it originally tripped. Further
troubleshooting and additional failure modes analysis by Entergy initially determined that
the cause of both events may have been a degraded resistor (R25) on the 23 EDG
automatic voltage regulator (AVR) card.
The 23 EDG AVR card was replaced, and the 23 EDG was again tested satisfactorily.
The voltage anomaly issues exhibited during the March 10, 2016, test were documented
in CR-IP2-2016-01430 which was closed in CR-IP2-2016-01260 to be included in the
causal assessment associated with the tripping of 23 EDG breaker on March 7, 2016.
Entergy assigned a vendor to perform laboratory bench testing and failure analysis of
the 23 EDG AVR card. The vendor report attributed the cause of the March 10, 2016,
loss of voltage control to a degraded solder joint on the AVR card. However, the vendor
report explicitly did not attribute the event on March 7, 2016, to the same cause.
Entergy assigned a corrective action in CR-IP2-2016-01260 to review the cause of the


Regulator Failure)  
                                                19
1R18 Plant Modifications (71111.18 - 2 samples)  
      23 EDG overcurrent trip on March 7, 2016, in light of the vendor report. The inspectors
      determined that the issue of concern remains open as a URI until this causal
Permanent Modifications  
      assessment has been completed by Entergy and assessed by NRC. (URI
.1 Control Rod Guide Tube Repairs in Location E-9
      05000247/2016001-06, 23 Emergency Diesel Generator Automatic Voltage
a. Inspection Scope  
      Regulator Failure)
The inspectors evaluated a modification to the reactor vessel upper internals to swap damaged control rod guide tube in location E-9 with abandoned guide tube in location  
1R18 Plant Modifications (71111.18 - 2 samples)
D-10. The inspectors verified that the design bases, licensing bases, and performance  
      Permanent Modifications
capability of the affected systems were not degraded by the modification. In addition,  
.1   Control Rod Guide Tube Repairs in Location E-9
the inspectors reviewed modification documents associated with the design change, including evaluation of equivalency and core flow changes, and post-modification testing. The inspectors also reviewed revisions to the affected drawings and interviewed  
  a. Inspection Scope
refueling and engineering personnel.  
      The inspectors evaluated a modification to the reactor vessel upper internals to swap
      damaged control rod guide tube in location E-9 with abandoned guide tube in location
      D-10. The inspectors verified that the design bases, licensing bases, and performance
      capability of the affected systems were not degraded by the modification. In addition,
      the inspectors reviewed modification documents associated with the design change,
      including evaluation of equivalency and core flow changes, and post-modification
      testing. The inspectors also reviewed revisions to the affected drawings and interviewed
      refueling and engineering personnel.
  b. Findings
      No findings were identified.
.2    Core Baffle-Former Bolt EC 64038
  a. Inspection Scope
      The inspectors reviewed EC 64038, IP2 Reactor Vessel Equivalent Replacement
      Baffle-to-Former Bolt. This modification was completed during RFO 2R22 and involved
      the replacement of 278 baffle-former bolts out of a total of 832 located in the Unit 2
      reactor vessel. Entergy replaced all of the bolts that were potentially degraded as
      observed by visual indications of a protruding bolt head or lock bar problem, bolts that
      did not pass UT, and bolts inaccessible for UT. Entergy staff also replaced 51 additional
      bolts that passed ultrasonic and visual examinations to increase the structural margin of
      the baffle-former assembly for future operating cycles.
      The inspectors reviewed the equivalency evaluation completed by Entergy staff to install
      baffle-former bolts of a different material and configuration than the original bolts. The
      inspectors reviewed the associated EC package to determine whether the replacement
      bolts form, fit, and function were maintained compared to the original bolts and whether
      the change conformed to the design and licensing bases of the baffle-former assembly.
      Specifically, this change involved replacing the original baffle-former bolts made of
      type 347 stainless steel with bolts made of type 316 stainless steel. The baffle-former
      bolt head configuration was also changed from an original internal hex and slot design
      (secured with a welded lock bar) to an external hex configuration with an integral locking
      cup design. The design change document further evaluated a more gradual fillet


b. Findings  
                                              20
No findings were identified.  
      geometry between the bolt head and shank intended to reduce the stress concentration
      at that transition and provide for improved fatigue resistance.
.2 Core Baffle-Former Bolt EC 64038
  b. Findings
a. Inspection Scope  
      No findings were identified.
The inspectors reviewed EC 64038, "IP2 Reactor Vessel Equivalent Replacement
1R19 Post-Maintenance Testing (71111.19 - 8 samples)
Baffle-to-Former Bolt."  This modification was completed during RFO 2R22 and involved
  a. Inspection Scope
the replacement of 278 baffle-former bolts out of a total of 832 located in the Unit 2
      The inspectors reviewed the post-maintenance tests for the maintenance activities listed
reactor vessel.  Entergy replaced all of the bolts that were potentially degraded as
      below to verify that procedures and test activities ensured system operability and
observed by visual indications of a protruding bolt head or lock bar problem, bolts that did not pass UT, and bolts inaccessible for UT. Entergy staff also replaced 51 additional bolts that passed ultrasonic and visual examinations to increase the structural margin of
      functional capability. The inspectors reviewed the test procedure to verify that the
the baffle-former assembly for future operating cycles.  
      procedure adequately tested the safety functions that may have been affected by the
      maintenance activity, that the acceptance criteria in the procedure was consistent with
      the information in the applicable licensing basis and/or design basis documents, and that
      the test results were properly reviewed and accepted and problems were appropriately
      documented. The inspectors also walked down the affected job site, observed the
      pre-job brief and post-job critique where possible, confirmed work site cleanliness was
      maintained, witnessed the test or reviewed test data to verify quality control hold points
      were performed and checked, and that results adequately demonstrated restoration of
      the affected safety functions.
      Unit 2
        21 EDG fuel oil transfer pump after planned maintenance on May 5, 2016
        Replacement of pressurizer level transmitters LT-459 and LT-460 on May 25, 2016
        21 CCW heat exchanger service water outlet weld repair on June 26, 2016
        Flux mapping system drive repairs following motor failures on June 28, 2016
      Unit 3
        Maintenance on service water components associated with the 32 EDG on May 5,
          2016 (this sample was part of an in-depth review of the EDG system)
        Modification of the 32 EDG space heaters on May 5, 2016 (this sample was part of
          an in-depth review of the EDG system)
        Maintenance on the 32 EDG air start system on May 6, 2016 (this sample was part
          of an in-depth review of the EDG system)
        Replacement of failed bistable LC-427K, steam generator 32 low level mismatch trip
          interlock, on May 18, 2016
  b. Findings
      No findings were identified.


                                                  21
The inspectors reviewed the equivalency evaluation completed by Entergy staff to install baffle-former bolts of a different material and configuration than the original bolts. The inspectors reviewed the associated EC package to determine whether the replacement
1R20 Refueling and Other Outage Activities (71111.20 - 2 samples)
bolts' form, fit, and function were maintained compared to the original bolts and whether
.1    Unit 2 RFO 2R22
the change conformed to the design and licensing bases of the baffle-former assembly. 
  a. Inspection Scope
Specifically, this change involved replacing the original baffle-former bolts made of type 347 stainless steel with bolts made of type 316 stainless steel. The baffle-former bolt head configuration was also changed from an original internal hex and slot design (secured with a welded lock bar) to an external hex configuration with an integral locking
      The inspectors reviewed the stations work schedule and outage risk plan for the Unit 2
cup design. The design change document further evaluated a more gradual fillet 
      maintenance during RFO 2R22, which was conducted from March 7, 2016, to June 16,
20  geometry between the bolt head and shank intended to reduce the stress concentration at that transition and provide for improved fatigue resistance.  
      2016. The inspectors reviewed Entergys development and implementation of outage
      plans and schedules to verify that risk, industry experience, previous site-specific
      problems, and defense-in-depth were considered. During the outage, the inspectors
      observed portions of the shutdown and cooldown processes and monitored controls
      associated with the following outage activities:
        Configuration management, including maintenance of defense-in-depth,
          commensurate with the outage plan for the key safety functions and compliance with
          the applicable TSs when taking equipment OOS
        Implementation of clearance activities and confirmation that tags were properly hung
          and that equipment was appropriately configured to safely support the associated
          work or testing
        Installation and configuration of reactor coolant pressure, level, and temperature
          instruments to provide accurate indication and instrument error accounting
        Status and configuration of electrical systems and switchyard activities to ensure that
          TSs were met
        Monitoring of decay heat removal operations
        Impact of outage work on the ability of the operators to operate the spent fuel pool
          cooling system
        Reactor water inventory controls, including flow paths, configurations, alternative
          means for inventory additions, and controls to prevent inventory loss
        Activities that could affect reactivity
        Maintenance of secondary containment as required by TSs
        Refueling activities, including fuel handling and fuel receipt inspections
        Fatigue management
        Tracking of startup prerequisites, walkdown of the primary containment to verify that
          debris had not been left which could block the ECCS suction strainers, and startup
          and ascension to full power operation
        Foreign Object Search and Retrieval for missing baffle bolts and locking tabs
        Identification and resolution of problems related to RFO activities
      During this outage, Entergy replaced 278 degraded baffle bolts in the Unit 2 reactor
      vessel baffle assembly. This emergent project resulted in the extension of the outage
      schedule from 30 days to 102 days.
  b. Findings
      Introduction. The inspectors identified a Green NCV of TS 5.4.1 for Entergys failure to
      implement procedure OAP-007, Containment Entry and Egress. Specifically, workers
      transiting the inner and outer crane wall sections of containment on June 11, 2016, failed
      to maintain at least one (of two) flow channeling gate closed to ensure availability of the
      containment sumps to provide suction for the ECCS.


b. Findings
                                          22
No findings were identified.
Description. On June 11, 2016, in mode 4, in preparation for reactor startup, Entergy
1R19 Post-Maintenance Testing (71111.19 - 8 samples)
was performing maintenance in containment required prior to mode 3, such as reactor
a. Inspection Scope
coolant pump motor balancing and steam flow transmitter troubleshooting. These
The inspectors reviewed the post-maintenance tests for the maintenance activities listed
activities required scaffolds to be temporarily erected for workers to safely perform
below to verify that procedures and test activities ensured system operability and  
maintenance. While transiting from the inner to outer section of containment, the
functional capability. The inspectors reviewed the test procedure to verify that the procedure adequately tested the safety functions that may have been affected by the maintenance activity, that the acceptance criteria in the procedure was consistent with
inspectors noted that both flow channeling gates were maintained open simultaneously
the information in the applicable licensing basis and/or design basis documents, and that
as workers carried scaffold poles and hardware out of the area.
the test results were properly reviewed and accepted and problems were appropriately
In the event of a postulated LOCA, Unit 2 relies on two sumps to provide a suction
documented. The inspectors also walked down the affected job site, observed the pre-job brief and post-job critique where possible, confirmed work site cleanliness was maintained, witnessed the test or reviewed test data to verify quality control hold points
source for the internal recirculation pumps and residual heat removal pumps,
were performed and checked, and that results adequately demonstrated restoration of
respectively, after the injection phase of the accident. The sumps have cylindrical
the affected safety functions.  
screens with large surface area and small holes to filter small debris and maintain
adequate net positive suction head for the associated pumps. The reactor cavity sump
and large intervening barriers prevent large debris generated from the accident, such as
insulation, from reaching and blocking the recirculation and containment sump screens.
Entergy procedure OAP-007, Containment Entry and Egress, precaution and limitation
step 2.30.2, states, In mode 1, 2, 3, or 4, entry inside the crane wall shall use the
double gate entry point via gates 17 and 23. One gate shall remain shut and secured at
all times to maintain flow channeling and sump operability. Securing gates requires a
padlock or nut and bolt closure from the outside. This will require posting a gate monitor
to allow exit. The inspectors noted, while a gate monitor was posted, both gates were
maintained open during passage and not secured with a padlock or nut and bolt closure.
Upon questioning by the inspectors, Entergy immediately coached the gate monitor and
restored the gates to an acceptable position. Entergy generated CR-IP2-2016-04036 to
address this issue.
Analysis. The inspectors determined that Energys failure to maintain either gate 17 or
gate 23 closed during passage in accordance with OAP-007 was a performance
deficiency. The performance deficiency was more than minor because it is associated
with the configuration control (shutdown equipment lineup) attribute and adversely
affected the Mitigating Systems cornerstone objective to ensure the availability,
reliability, and capability of systems that respond to initiating events to prevent
undesirable consequences (i.e., core damage). The inspectors evaluated the finding in
accordance with IMC 0609, Appendix G, Attachment 1, Exhibit 3, and determined that a
detailed risk evaluation was necessary because the finding represented a loss of system
safety function. A detailed risk assessment was conducted conservatively assuming
complete failure of the recirculation and containment sumps due to the performance
deficiency. Given that Unit 2 was in mode 4, in plant operating state 1, with a late time
window, the at-power simplified plant analysis risk model for large-break LOCAs was
determined to best model the degrade condition and plant response. An exposure time
of one day was assumed. No credit was assumed for the decrease in energy that would
be anticipated in a release during a LOCA in mode 4, nor the corresponding reduction in
debris generation. This was also considered conservative. Utilizing Systems Analysis
Program for Hands-On Integrated Reliability Evaluation, version 8.13, with Indian Point
Unit 2 Simplified Plant Analysis Risk Model, version 8.19, for the assumed conditions,
the change in core damage frequency was determined to be 7E-9. Therefore, this issue
represents a Green finding.


                                                  23
Unit 2   21 EDG fuel oil transfer pump after planned maintenance on May 5, 2016  Replacement of pressurizer level transmitters LT-459 and LT-460 on May 25, 2016  21 CCW heat exchanger service water outlet weld repair on June 26, 2016 Flux mapping system drive repairs following motor failures on June 28, 2016
      This finding had a cross-cutting aspect in the area of Human Performance, Avoid
Unit 3  Maintenance on service water components associated with the 32 EDG on May 5, 2016 (this sample was part of an in-depth review of the EDG system) Modification of the 32 EDG space heaters on May 5, 2016 (this sample was part of an in-depth review of the EDG system)  Maintenance on the 32 EDG air start system on May 6, 2016 (this sample was part of an in-depth review of the EDG system)  Replacement of failed bistable LC-427K, steam generator 32 low level mismatch trip interlock, on May 18, 2016
      Complacency, because Entergy did not consider potential undesired consequences of
b. Findings
      actions before performing work and implement appropriate error-reduction tools.
      Specifically, the work crew did not understand the requirements and potential
No findings were identified.
      consequences prior to commencing work and the gate monitor did not enforce these
      requirements to maintain at least one gate locked or pinned closed as required by
      OAP-007. [H.12]
      Enforcement. Unit 2 TS 5.4.1.a requires that the procedures listed in Attachment A to
      Regulatory Guide 1.33, Quality Assurance Program Requirements, Revision 2, be
      established and implemented. Attachment A states that instructions should be prepared,
      as appropriate, for access to containment and changing modes of operation of the
      ECCS. Entergy procedure OAP-007, Containment Entry and Egress, Step 2.30.2,
      states, In mode 1, 2, 3, or 4, entry inside the crane wall shall use the double gate entry
      point via gates 17 and 23. One gate shall remain shut and secured at all times to
      maintain flow channeling and sump operability. Securing gates requires a padlock or nut
      and bolt closure from the outside. Contrary to the above, on June 11, 2016, Entergy did
      not maintain one gate secured at all times with a padlock or nut and bolt closure.
      Entergy entered this issue into the CAP as CR-IP2-2016-04036. Because this violation
      was of very low safety significance (Green), and Entergy entered this performance
      deficiency into the CAP, the NRC is treating this as a NCV in accordance with
      Section 2.3.2.a of the NRC Enforcement Policy. (NCV 05000247/2016002-03, Failure
      to Maintain Flow Channeling Gates Closed in Accordance with the Containment
      Procedure)
.2    Unit 2 Forced Outage
  a. Inspection Scope
      Unit 2 conducted a forced outage from June 24 to 27, 2016, in order to complete weld
      repairs on a through-wall leak on the service water inlet line to the 21 CCW heat
      exchanger. These repairs required shutting down to mode 4 in order to meet the
      TS 3.7.7, Component Cooling Water (CCW) System, limiting condition for operations
      for CCW operability. While these repairs were being completed, the grid operator
      completed repairs to breaker 9 in the offsite switchyard. During the outage, the
      inspectors observed portions of the shutdown and cooldown processes and monitored
      controls associated with the following outage activities:
        Configuration management, including maintenance of defense-in-depth,
          commensurate with the outage plan for the key safety functions and compliance with
          the applicable TSs when taking equipment OOS
        Implementation of clearance activities and confirmation that tags were properly hung
          and that equipment was appropriately configured to safely support the associated
          work or testing
        Status and configuration of electrical systems and switchyard activities to ensure that
          TSs were met
        Monitoring of decay heat removal operations
        Reactor water inventory controls, including flow paths, configurations, alternative
          means for inventory additions, and controls to prevent inventory loss
        Activities that could affect reactivity


   
                                                24
21  1R20 Refueling and Other Outage Activities (71111.20 - 2 samples)  
          Tracking of startup prerequisites
.1 Unit 2 RFO 2R22
          Identification and resolution of problems related to RFO activities
a. Inspection Scope  
      When all repairs had been completed, Entergy restarted Unit 2 on June 27, 2016.
The inspectors reviewed the station's work schedule and outage risk plan for the Unit 2
  b. Findings
maintenance during RFO 2R22, which was conducted from March 7, 2016, to June 16,  
      No findings were identified.
2016. The inspectors reviewed Entergy's development and implementation of outage plans and schedules to verify that risk, industry experience, previous site-specific problems, and defense-in-depth were considered. During the outage, the inspectors  
1R22 Surveillance Testing (71111.22 - 6 samples)
observed portions of the shutdown and cooldown processes and monitored controls
  a. Inspection Scope
associated with the following outage activities:  
      The inspectors observed performance of surveillance tests and/or reviewed test data of
  Configuration management, including maintenance of defense-in-depth, commensurate with the outage plan for the key safety functions and compliance with the applicable TSs when taking equipment OOS  Implementation of clearance activities and confirmation that tags were properly hung and that equipment was appropriately configured to safely support the associated
      selected risk-significant SSCs to assess whether test results satisfied TSs, the UFSAR,
work or testing  Installation and configuration of reactor coolant pressure, level, and temperature instruments to provide accurate indication and instrument error accounting  Status and configuration of electrical systems and switchyard activities to ensure that
      and Entergys procedure requirements. The inspectors verified that test acceptance
TSs were met  Monitoring of decay heat removal operations  Impact of outage work on the ability of the operators to operate the spent fuel pool cooling system  Reactor water inventory controls, including flow paths, configurations, alternative means for inventory additions, and controls to prevent inventory loss  Activities that could affect reactivity  Maintenance of secondary containment as required by TSs  Refueling activities, including fuel handling and fuel receipt inspections  Fatigue management  Tracking of startup prerequisites, walkdown of the primary containment to verify that debris had not been left which could block the ECCS suction strainers, and startup and ascension to full power operation  Foreign Object Search and Retrieval for missing baffle bolts and locking tabs  Identification and resolution of problems related to RFO activities
      criteria were clear, tests demonstrated operational readiness and were consistent with
During this outage, Entergy replaced 278 degraded baffle bolts in the Unit 2 reactor
      design documentation, test instrumentation had current calibrations and the range and
vessel baffle assembly.  This emergent project resulted in the extension of the outage schedule from 30 days to 102 days.
      accuracy for the application, tests were performed as written, and applicable test
b. Findings
      prerequisites were satisfied. Upon test completion, the inspectors considered whether
Introduction.  The inspectors identified a Green NCV of TS 5.4.1 for Entergy's failure to implement procedure OAP-007, "Containment Entry and Egress."  Specifically, workers transiting the inner and outer crane wall sections of containment on June 11, 2016, failed
      the test results supported that equipment was capable of performing the required safety
to maintain at least one (of two) flow channeling gate closed to ensure availability of the  
      functions. The inspectors reviewed the following surveillance tests:
containment sumps to provide suction for the ECCS. 
      Unit 2
22    Description.  On June 11, 2016, in mode 4, in preparation for reactor startup, Entergy was performing maintenance in containment required prior to mode 3, such as reactor coolant pump motor balancing and steam flow transmitter troubleshooting.  These activities required scaffolds to be temporarily erected for workers to safely perform
          WO 446385, 21 EDG AVR card inspection, on May 24, 2016
maintenance. While transiting from the inner to outer section of containment, the
          2-PT-Q013 for containment isolation valve 851B (22 safety injection (SI) pump tie to
inspectors noted that both flow channeling gates were maintained open simultaneously
          23 SI pump discharge) on June 6, 2016
as workers carried scaffold poles and hardware out of the area. 
          2-PT-Q029B quarterly in-service surveillance test for the 22 SI pump on June 6,
          2016
      Unit 3
          3-PT-M079B 32 EDG monthly surveillance on May 30, 2016 (this sample was part of
          an in-depth review of the EDG system)
          34 steam generator pressure instrument channel check on June 21, 2016
          0-SOP-LEAKRATE-001, RCS Leakrate Surveillance, Evaluation and Leak
          Identification, beginning on June 28, 2016
  b. Findings
      No findings were identified.
      Cornerstone: Emergency Preparedness


In the event of a postulated LOCA, Unit 2 relies on two sumps to provide a suction source for the internal recirculation pumps and residual heat removal pumps,
                                                25
respectively, after the injection phase of the accident. The sumps have cylindrical
1EP6 Drill Evaluation (71114.06 - 1 sample)
screens with large surface area and small holes to filter small debris and maintain
      Training Observations
adequate net positive suction head for the associated pumps. The reactor cavity sump and large intervening barriers prevent large debris generated from the accident, such as insulation, from reaching and blocking the recirculation and containment sump screens.  
  a. Inspection Scope
      The inspectors evaluated the conduct of Entergys ingestion pathway emergency
      preparedness drill on April 19, 2016, to identify any weaknesses and deficiencies in the
      classification, notification, and protective action recommendation development activities.
      The inspectors observed emergency response operations in the emergency operations
      facility to determine whether the event classification, notifications, and protective action
      recommendations were performed in accordance with procedures. The inspectors also
      attended the facility drill critique to compare inspector observations with those identified
      by Entergy staff in order to evaluate Entergys critique and to verify whether the staff was
      properly identifying weaknesses and entering them into the CAP.
  b. Findings
      No findings were identified.
2.    RADIATION SAFETY
      Cornerstone: Public Radiation Safety and Occupational Radiation Safety
2RS1 Radiological Hazard Assessment and Exposure Controls (71124.01)
  a. Inspection Scope
      During May 10-12 and June 13-17, 2016, the inspectors reviewed Entergys
      performance in assessing the radiological hazards and exposure control in the
      workplace. The inspectors used the requirements in 10 CFR 20, TSs, applicable
      industry standards, and procedures required by TSs as criteria for determining
      compliance.
      Radiological Hazards Control and Work Coverage
      The inspectors reviewed:
        Ambient radiological conditions during tours of the radiological controlled area,
          posted surveys, radiation work permits, adequacy of radiological controls, radiation
          protection job coverage, and contamination controls
        Controls for highly activated or contaminated materials stored within spent fuel pools
        Posting and physical controls for high radiation areas and very high radiation areas
  b. Findings
      No findings were identified.


                                              26
Entergy procedure OAP-007, "Containment Entry and Egress," precaution and limitation
2RS2 Occupational As Low As Is Reasonably Achievable (ALARA) Planning and Controls
step 2.30.2, states, "In mode 1, 2, 3, or 4, entry inside the crane wall shall use the double gate entry point via gates 17 and 23. One gate shall remain shut and secured at all times to maintain flow channeling and sump operability. Securing gates requires a  
      (71124.02)
padlock or nut and bolt closure from the outside. This will require posting a gate monitor
  a. Inspection Scope
to allow exit.The inspectors noted, while a gate monitor was posted, both gates were
      During May 10-12 and June 13-17, 2016, the inspectors assessed performance with
maintained open during passage and not secured with a padlock or nut and bolt closure.
      respect to maintaining occupational individual and collective radiation exposures ALARA.
Upon questioning by the inspectors, Entergy immediately coached the gate monitor and restored the gates to an acceptable position. Entergy generated CR-IP2-2016-04036 to address this issue. 
      The inspectors used the requirements in 10 CFR 20, TSs, applicable industry standards,
      and procedures required by TSs as criteria for determining compliance.
      Radiological Work Planning
      The inspectors reviewed:
        ALARA work activity evaluations, exposure estimates, and exposure mitigation
          requirements
        ALARA work planning, use of dose mitigation features and dose goals
        Work planning and the integration of ALARA requirements
  b. Findings
      No findings were identified.
2RS7 Radiological Environmental Monitoring Program (REMP) (71124.07 - 3 samples)
  a. Inspection Scope
      The inspectors reviewed the REMP to validate the effectiveness of the radioactive
      gaseous and liquid effluent release program and implementation of the groundwater
      protection initiative (GPI). The inspectors used the requirements in 10 CFR 20,
      40 CFR 190, 10 CFR 50, Appendix I, TSs, offsite dose calculation manual (ODCM),
      Nuclear Energy Institute 07-07, and procedures required by TSs as criteria for
      determining compliance.
      Inspection Planning
      The inspectors reviewed Entergys 2014 and 2015 annual radiological environmental
      and effluent monitoring reports, REMP program audits, ODCM changes, land use
      census, the UFSAR, and inter-laboratory comparison program results.
      Site Inspection
      The inspectors walked down various thermoluminescent dosimeter and air and water
      sampling locations and reviewed associated calibration and maintenance records. The
      inspectors observed the sampling of various environmental media as specified in the
      ODCM and reviewed any anomalous environmental sampling events including
      assessment of any positive radioactivity results. The inspectors reviewed any changes
      to the ODCM. The inspectors verified the operability and calibration of the
      meteorological tower instruments and meteorological data readouts. The inspectors
      reviewed environmental sample laboratory analysis results, laboratory instrument
      measurement detection sensitivities, laboratory quality control program audit results, and


                                                27
Analysis. The inspectors determined that Energy's failure to maintain either gate 17 or gate 23 closed during passage in accordance with OAP-007 was a performance deficiency. The performance deficiency was more than minor because it is associated with the configuration control (shutdown equipment lineup) attribute and adversely
      the inter- and intra-laboratory comparison program results. The inspectors reviewed the
affected the Mitigating Systems cornerstone objective to ensure the availability,  
      groundwater monitoring program as it applies to selected potential leaking SSCs.
reliability, and capability of systems that respond to initiating events to prevent
      GPI Implementation
undesirable consequences (i.e., core damage).  The inspectors evaluated the finding in
      The inspectors reviewed groundwater monitoring results, changes to the GPI program
accordance with IMC 0609, Appendix G, Attachment 1, Exhibit 3, and determined that a detailed risk evaluation was necessary because the finding represented a loss of system safety function.  A detailed risk assessm
      since the last inspection, anomalous results or missed groundwater samples, leakage or
ent was conducted conservatively assuming complete failure of the recirculation and containment sumps due to the performance
      spill events including entries made into the decommissioning files (10 CFR 50.75(g)),
deficiency.  Given that Unit 2 was in mode 4, in plant operating state 1, with a late time
      evaluations of surface water discharges, and Entergys evaluation of any positive
window, the at-power simplified plant analysis risk model for large-break LOCAs was determined to best model the degrade condition and plant response.  An exposure time of one day was assumed.  No credit was assumed for the decrease in energy that would
      groundwater sample results including appropriate stakeholder notifications and effluent
be anticipated in a release during a LOCA in mode 4, nor the corresponding reduction in  
      reporting requirements.
debris generation.  This was also considered conservative.  Utilizing Systems Analysis
      Identification and Resolution of Problems
Program for Hands-On Integrated Reliability Evaluation, version 8.13, with Indian Point Unit 2 Simplified Plant Analysis Risk Model, version 8.19, for the assumed conditions, the change in core damage frequency was determined to be 7E-9.  Therefore, this issue represents a Green finding.
      The inspectors evaluated whether problems associated with the REMP were identified at
      an appropriate threshold and properly addressed in Entergys CAP.
    b. Findings
      No findings were identified.
4.     OTHER ACTIVITIES
4OA1 Performance Indicator Verification (71151 - 6 samples)
      Initiating Events Performance Indicators
  aInspection Scope
      The inspectors reviewed Entergys submittals for the following Initiating Events
      cornerstone performance indicators for the period April 1, 2015, to March 31, 2016:
      Unit 2
          Unplanned scrams per 7000 critical hours (IE01)
          Unplanned power changes per 7000 critical hours (IE03)
          Unplanned scrams with complications (IE04)
      Unit 3
          Unplanned scrams (IE01)
          Unplanned power changes (IE03)
          Unplanned scrams with complications (IE04)
      To determine the accuracy of the performance indicator data reported during those
      periods, inspectors used definitions and guidance contained in Nuclear Energy
      Institute 99-02, Regulatory Assessment Performance Indicator Guideline, Revision 7.
      The inspectors reviewed Entergys operator narrative logs, maintenance planning
      schedules, CRs, event reports, and NRC integrated inspection reports to validate the


 
                                                28
23  This finding had a cross-cutting aspect in the area of Human Performance, Avoid Complacency, because Entergy did not consider potential undesired consequences of
      accuracy of the submittals. There were no unplanned power changes or scrams with
actions before performing work and implement appropriate error-reduction tools. Specifically, the work crew did not understand the requirements and potential consequences prior to commencing work and the gate monitor did not enforce these
      complications during the review period.
requirements to maintain at least one gate locked or pinned closed as required by
  b. Findings
OAP-007. [H.12]
      No findings were identified.
4OA2 Problem Identification and Resolution (71152 - 4 samples)
.1    Routine Review of Problem Identification and Resolution Activities
  a. Inspection Scope
      As required by Inspection Procedure 71152, Problem Identification and Resolution, the
      inspectors routinely reviewed issues during baseline inspection activities and plant
      status reviews to verify that Entergy entered issues into the CAP at an appropriate
      threshold, gave adequate attention to timely corrective actions, and identified and
      addressed adverse trends. In order to assist with the identification of repetitive
      equipment failures and specific human performance issues for follow up, the inspectors
      performed a daily screening of items entered into the CAP and periodically attended CR
      screening meetings. The inspectors also confirmed, on a sampling basis, that, as
      applicable, for identified defects and non-conformances, Entergy performed an
      evaluation in accordance with 10 CFR 21.
  b. Findings
      No findings were identified.
.2    Semi-Annual Trend Review
  a. Inspection Scope
      The inspectors performed a semi-annual review of site issues, as required by Inspection
      Procedure 71152, Problem Identification and Resolution, to identify trends that might
      indicate the existence of more significant safety issues. In this review, the inspectors
      included repetitive or closely-related issues that may have been documented by Entergy
      outside of the CAP, such as trend reports, performance indicators, major equipment
      problem lists, system health reports, maintenance rule assessments, and maintenance
      or CAP backlogs. The inspectors also reviewed Entergys CAP database for the first
      and second quarters of 2016 to assess CRs written in various subject areas (equipment
      problems, human performance issues, etc.), as well as individual issues identified during
      the NRCs daily CR review (Section 4OA2.1). The inspectors reviewed the Entergy
      quarterly trend report for the first quarter of 2016 to verify that Entergy was appropriately
      evaluating and trending adverse conditions in accordance with applicable procedures.
  b. Findings and Observations
      No findings were identified.
      The inspectors identified a trend in work being performed that was contrary to written
      work instructions and procedures, and work packages had been closed out without


                                            29
Enforcement.  Unit 2 TS 5.4.1.a requires that the procedures listed in Attachment A to Regulatory Guide 1.33, "Quality Assurance Program Requirements," Revision 2, be
documenting the deviation from the work order. While reviewing completed work order
established and implemented. Attachment A states that instructions should be prepared,
WO 447966 Task 10, Internal Coating Repair for 21 CCW HX, the inspectors found a
as appropriate, for access to containment and changing modes of operation of the  
note in the work order stating that the internal coating repair to the pipe had not been
ECCS. Entergy procedure OAP-007, "Containment Entry and Egress," Step 2.30.2,
done in accordance with the engineering change. The engineering change had been
states, "In mode 1, 2, 3, or 4, entry inside the crane wall shall use the double gate entry point via gates 17 and 23.  One gate shall remain shut and secured at all times to maintain flow channeling and sump operability. Securing gates requires a padlock or nut
written when the coating repair was expected to be small, but the actual area that was
and bolt closure from the outside."  Contrary to the above, on June 11, 2016, Entergy did
recoated was much larger. A larger area of coating increases the impact on the heat
not maintain one gate secured at all times with a padlock or nut and bolt closure. 
exchanger if the coating were to flake off and block the flow of service water. The work
Entergy entered this issue into the CAP as CR-IP2-2016-04036. Because this violation was of very low safety significance (Green), and Entergy entered this performance deficiency into the CAP, the NRC is treating this as a NCV in accordance with
package was closed and no condition report was written. This performance deficiency is
Section 2.3.2.a of the NRC Enforcement Policy.  (NCV 05000247/2016002-03, Failure to Maintain Flow Channeling Gates Closed in Accordance with the Containment
minor because the coating was applied with procedurally directed quality controls and
Procedure)
the likelihood that it would flake off is very small; and is the same as the original smaller
 
area specified in the work package. However, the work package was closed without
.2 Unit 2 Forced Outage
documenting the deviation and no CR was written.
a. Inspection Scope
In another example, the inspectors noted that WO 412920 Task 15 to perform a surge
Unit 2 conducted a forced outage from June 24 to 27, 2016, in order to complete weld repairs on a through-wall leak on the service water inlet line to the 21 CCW heat
test on 11 centrifugal air compressor (CENTAC) after overhaul was completed on
exchanger.  These repairs required shutting down to mode 4 in order to meet the TS 3.7.7, "Component Cooling Water (CCW) System," limiting condition for operations
December 22, 2015. However, the completion notes and documentation for the task
for CCW operability.  While these repairs were being completed, the grid operator
showed that the test was unable to be performed due to a test equipment problem. The
completed repairs to breaker 9 in the offsite switchyard.  During the outage, the  
work package was closed and no CR was written. Subsequently, after being returned to
inspectors observed portions of the shutdown and cooldown processes and monitored controls associated with the following outage activities:
service, the compressor failed in service due to multiple surging events on January 7,
  Configuration management, including maintenance of defense-in-depth, commensurate with the outage plan for the key safety functions and compliance with the applicable TSs when taking equipment OOS  Implementation of clearance activities and confirmation that tags were properly hung and that equipment was appropriately configured to safely support the associated
2016. Troubleshooting under WO 433939 revealed that the motor high load limit had not
work or testing  Status and configuration of electrical systems and switchyard activities to ensure that
been adjusted to account for the increased load due to reduced compressor clearances
TSs were met  Monitoring of decay heat removal operations  Reactor water inventory controls, including flow paths, configurations, alternative means for inventory additions, and controls to prevent inventory loss  Activities that could affect reactivity 
introduced by the overhaul. This performance deficiency is screened to minor because
24    Tracking of startup prerequisites
the 11 CENTAC is not a safety-related piece of equipment and would not affect the MC
  Identification and resolution of problems related to RFO activities
0609 cornerstone thresholds or other generic criteria. Unit 2 and Unit 3 have dedicated
  When all repairs had been completed, Entergy restarted Unit 2 on June 27, 2016.  
instrument air compressors that are credited in the FSAR to respond to a loss of
instrument air event. If the 11 CENTAC (located in Unit 1) were to fail, the unit-specific
IACs would automatically start to prevent a loss of instrument air at both Units 2 and 3.
A third recent example of work being performed contrary to written instructions occurred
during 2RFO22 when the inspectors identified that the workers deviated from the
surveillance procedure by demonstrating the installation of the emergency containment
hatch plug without properly inflating the plug seals as directed by the procedure. This
performance deficiency was previously documented in a prior inspection report as non-
cited violation 05000247/05000286/2016001-02, Failure to Adequately Implement Risk
Management Actions for the Containment Key Safety Function.
In all cases, the deviations from written work instructions were directed by Entergy
supervision. In addition, the inspectors noted that Entergy had self-identified similar
observations where work packages or condition reports had been closed without fully
completing the specified actions including CR-IP2-2015-05833, CR-IP2-2016-00103,
CR-IP3-2015-04729, CR-IP3-2016-00072, CR-IP3-2016-00075, and CR-IP3-2015-
04019. These CRs are further examples of work orders that were closed with deviations
that were not documented or resolved. Nuclear Oversight had identified several of these
condition reports. Entergy has taking immediate corrective action in response to these
performance deficiencies.


b. Findings
                                                30
  No findings were identified.
.3    Annual Sample: Maintenance Rule Self-Assessment of Corrective Actions
1R22 Surveillance Testing (71111.22
  a. Inspection Scope
- 6 samples)
      The inspectors performed an in-depth review of Entergys corrective actions associated
a. Inspection Scope  
      with self-assessment LO-IP3LO-2015-72, Maintenance Rule (a)(3) Assessment. The
The inspectors observed performance of surveillance tests and/or reviewed test data of  
      self-assessment was performed to satisfy both the self-assessment criteria in EN-LI-104,
selected risk-significant SSCs to assess whether test results satisfied TSs, the UFSAR,  
      Self-Assessment and Benchmark Process, and the maintenance rule periodic
and Entergy's procedure requirements. The inspectors verified that test acceptance criteria were clear, tests demonstrated operational readiness and were consistent with design documentation, test instrumentation had current calibrations and the range and  
      assessment criteria in EN-DC-207.
accuracy for the application, tests were performed as written, and applicable test
      The inspectors assessed Entergys problem identification threshold, extent of condition
prerequisites were satisfied.  Upon test completion, the inspectors considered whether  
      reviews, and the prioritization and timeliness of Entergy corrective actions to determine
the test results supported that equipment was capable of performing the required safety
      whether Entergy was appropriately identifying, characterizing, and correcting problems
functions. The inspectors reviewed the following surveillance tests:
      associated with this issue and whether the planned or completed corrective actions were
Unit 2  WO 446385, 21 EDG AVR card inspection, on May 24, 2016  2-PT-Q013 for containment isolation valve 851B (22 safety injection (SI) pump tie to 23 SI pump discharge) on June 6, 2016  2-PT-Q029B quarterly in-service surveillance test for the 22 SI pump on June 6, 2016 
      appropriate. The inspectors compared the actions taken to the requirements of
Unit 3  3-PT-M079B 32 EDG monthly surveillance on May 30, 2016 (this sample was part of an in-depth review of the EDG system)  34 steam generator pressure instrument channel check on June 21, 2016  0-SOP-LEAKRATE-001, RCS Leakrate Surveillance, Evaluation and Leak Identification, beginning on June 28, 2016
      Entergys CAP and 10 CFR 50, Appendix B. In addition, the inspectors interviewed
b. Findings  
      engineering personnel to assess the effectiveness of the implemented corrective
  No findings were identified.
      actions.
  Cornerstone:  Emergency Preparedness
  b. Findings and Observations
   
      No findings were identified.
25  1EP6 Drill Evaluation (71114.06 - 1 sample)
      Entergy identified three standard deficiencies during their self-assessment and wrote
  Training Observations
      CRs to document each one. One of the standard deficiencies was that the maintenance
a. Inspection Scope
      rule basis documents were not being reviewed at least once every two years as required
The inspectors evaluated the conduct of Entergy's ingestion pathway emergency
      by procedure EN-DC-204, Maintenance Rule Scope and Basis. The purpose of this
preparedness drill on April 19, 2016, to identify any weaknesses and deficiencies in the  
      review was to ensure that the documents were updated if the configuration of the system
classification, notification, and protective action recommendation development activities. The inspectors observed emergency response
      changed or if the performance criteria needed to be adjusted. Entergy wrote CR-IP3-
operations in the emergency operations facility to determine whether the event classification, notifications, and protective action
      2015-03628 and assigned a corrective action to create work trackers to perform the
recommendations were performed in accordance with procedures.  The inspectors also
      basis document reviews. They chose to use work trackers instead of corrective actions
attended the facility drill critique to compare inspector observations with those identified
      under the CAP because the work had historically been assigned using work trackers.
by Entergy staff in order to evaluate Entergy's critique and to verify whether the staff was properly identifying weaknesses and entering them into the CAP.  
      However, because work trackers do not receive the same priority as corrective actions,
b. Findings
      some of the maintenance rule basis documents had still not been reviewed at the time of
No findings were identified.  
      this inspection, over a year after the completion of the self-assessment. The inspectors
2. RADIATION SAFETY
      determined that this was not a more than minor issue because the systems in question
   Cornerstone: Public Radiation Safety and Occupational Radiation Safety
      did not show signs of inadequate maintenance.
2RS1 Radiological Hazard Assessment and Exposure Controls (71124.01)
.4   Annual Sample: Unit 2 Reactor Trip on December 5, 2015
a. Inspection Scope  
  a. Inspection Scope
During May 10-12 and June 13-17, 2016, the inspectors reviewed Entergy's
      The inspectors performed an in-depth review of Entergys evaluations and corrective
performance in assessing the radiological hazards and exposure control in the workplace.  The inspectors used the requirements in 10 CFR 20, TSs, applicable industry standards, and procedures required by TSs as criteria for determining
      actions associated with CR-IP2-2015-05484 and the related apparent cause evaluation
compliance.
      for the December 5, 2015, manual reactor trip in response to indications of multiple
Radiological Hazards Control and Work Coverage
      dropped control rods caused by the loss of control rod power due to a power supply
The inspectors reviewed:
      failure. Entergy performed an apparent cause evaluation and determined the direct
  Ambient radiological conditions during tours of the radiological controlled area, posted surveys, radiation work permits, adequacy of radiological controls, radiation protection job coverage, and contamination controls  Controls for highly activated or contaminated materials stored within spent fuel pools  Posting and physical controls for high radiation areas and very high radiation areas
      cause of the event was the loss of motor control center (MCC)-24 due to an internal fault
b. Findings
      at the line side leads at cubicle 2H where they connect to the bucket stab assemblies.
      The apparent cause was an unanticipated loss of power to the control rod system due to
No findings were identified. 
      the degradation of the primary control rod power supply (PS1) which failed to function for
   
26  2RS2 Occupational As Low As Is Reasonably Achievable (ALARA) Planning and Controls
(71124.02)
a. Inspection Scope 
During May 10-12 and June 13-17, 2016, the inspectors assessed performance with
respect to maintaining occupational individual and collective radiation exposures ALARA.
The inspectors used the requirements in 10 CFR 20, TSs, applicable industry standards,
and procedures required by TSs as criteria for determining compliance. 
Radiological Work Planning
The inspectors reviewed:


  ALARA work activity evaluations, exposure estimates, and exposure mitigation
                                                31
requirements  ALARA work planning, use of dose mitigation features and dose goals  Work planning and the integration of ALARA requirements 
      more than 10 minutes when the operating alternate power supply (PS2) was
b. Findings  
      deenergized.
No findings were identified.
      The inspectors assessed Entergys problem identification threshold, problem analysis,
      extent of condition reviews, compensatory actions, and the prioritization and timeliness
2RS7 Radiological Environmental Monitoring Program (REMP) (71124.07 - 3 samples)
      of Entergy's corrective actions to determine whether Entergy was appropriately
a. Inspection Scope
      identifying, characterizing, and correcting problems associated with this issue and
The inspectors reviewed the REMP to validate the effectiveness of the radioactive
      whether the planned or completed corrective actions were appropriate. The inspectors
gaseous and liquid effluent release program and implementation of the groundwater
      compared the actions taken to the requirements of Entergy's CAP and 10 CFR 50,
protection initiative (GPI). The inspectors used the requirements in 10 CFR 20,  
      Appendix B, Criterion XVI, Corrective Action.
40 CFR 190, 10 CFR 50, Appendix I, TSs, offsite dose calculation manual (ODCM), Nuclear Energy Institute 07-07, and procedures required by TSs as criteria for determining compliance.  
  b. Findings and Observations
      No findings were identified.
      The inspectors found that Entergy took appropriate actions to identify the direct and
      apparent cause of the issue. The direct cause of the event was the loss of MCC-24 due
      to an internal fault at the line side leads at cubicle 2H where they connect to the bucket
      stab assemblies. The apparent cause was an unanticipated loss of power to the control
      rod system due to the degradation of the primary control rod PS1, which failed to
      function when PS2 was lost. Entergy replaced the degraded rod control PS1; and the
      MCC-24 compartments were removed to facilitate inspection and testing of the MCC
      bus, control wires, and MCC internal. PS2 was also restored to operation after the fault
      was cleared.
      The inspector determined that the internal electrical fault that deenergized PS2 and the
      prior degradation in PS1 was not within Entergys ability to foresee and prevent.
      Therefore, there was no performance deficiency identified. Entergys overall response to
      the issue was commensurate with the safety significance, was timely, and the actions
      taken and planned were reasonable to resolve the failure of the primary control rod PS1.
.5    Annual Sample: Unexpected Number of Degraded Baffle-Former Bolts Discovered in
      the Unit 2 Reactor Pressure Vessel
  a. Inspection Scope
      The inspectors performed an in-depth review of Entergys root cause evaluation and
      corrective actions associated with CR-IP2-2016-02348 for baffle-former (baffle) bolts
      found with indications of degradation during the Indian Point Unit 2 RFO 2R22. Entergy
      performed ultrasonic examinations of the baffle bolts in accordance with their procedures
      as part of a planned activity. After an unexpected number of degraded baffle bolts were
      discovered, Entergy staff reported the issue to the NRC as Event Notification No. 51829
      on March 29, 2016, because the as-found number and location of degraded bolts
      represented an unanalyzed condition. Entergy staff completed corrective actions to
      replace all of the potentially degraded baffle bolts on Unit 2. Entergy staff further
      replaced a population of additional bolts that exhibited no indications of degradation and
      performed an evaluation to determine the potential for baffle bolt failures at Unit 3.
      The baffle-former bolts help secure vertical plates (also referred to as baffle plates)
      inside the reactor vessel, which then forms a structure surrounding the reactor fuel
      assemblies to orient the fuel and to direct coolant flow through the core. A sufficient


  Inspection Planning
                                              32
The inspectors reviewed Entergy's 2014 and 2015 annual radiological environmental and effluent monitoring reports, REMP program audits, ODCM changes, land use
  number of baffle bolts are required to remain intact to secure the baffle plates in place so
census, the UFSAR, and inter-laboratory comparison program results.  
  as to not affect control rod insertion or impede emergency core cooling flow during
  postulated accident conditions. Bolt heads that separate and are no longer held in place
Site Inspection 
  by bolt lock-tabs can also become a loose parts concern.
The inspectors walked down various thermoluminescent dosimeter and air and water
  The inspectors determined whether Entergys acceptable baffle bolt pattern analysis for
sampling locations and reviewed associated calibration and maintenance records. The  
  Unit 2 was completed in accordance with the NRC-approved methodology and provided
inspectors observed the sampling of various environmental media as specified in the  
  appropriate structural margin for the next cycle of operation to ensure the Unit 2 baffle
ODCM and reviewed any anomalous environmental sampling events including assessment of any positive radioactivity results. The inspectors reviewed any changes to the ODCM. The inspectors verified the operability and calibration of the meteorological tower instruments and meteorological data readouts. The inspectors  
  plates will remain in place during both normal operation and limiting postulated accident
reviewed environmental sample laboratory analysis results, laboratory instrument
  conditions. The inspectors further determined whether Entergys evaluations of the
measurement detection sensitivities, laboratory quality control program audit results, and
  baffle bolts installed in Indian Point Unit 3 were technically sufficient to conclude the
27  the inter- and intra-laboratory comparison program results. The inspectors reviewed the groundwater monitoring program as it applies to selected potential leaking SSCs.
  Unit 3 baffle assembly will perform as intended until the next planned RFO, at which time
GPI Implementation  The inspectors reviewed groundwater monitoring results, changes to the GPI program since the last inspection, anomalous results or missed groundwater samples, leakage or
  Entergy plans to examine the bolts. The inspectors reviewed Entergys procedures for
spill events including entries made into the decommissioning files (10 CFR 50.75(g)),
  determining the functionality and operability of degraded SSC as they relate to Unit 3.
evaluations of surface water discharges, and Entergy's evaluation of any positive
  The inspectors further interviewed Entergy engineering personnel and contractor staff to
groundwater sample results including appropriate stakeholder notifications and effluent reporting requirements. 
  discuss the results of Entergys technical evaluations and to assess the effectiveness of
  Identification and Resolution of Problems 
  the implemented and planned corrective actions.
The inspectors evaluated whether problems associated with the REMP were identified at
  The inspectors assessed Entergys problem identification threshold, cause analyses,
an appropriate threshold and properly addressed in Entergy's CAP.  
  extent of condition, compensatory actions, and the prioritization and timeliness of
b. Findings  
  Entergys corrective actions to determine whether Entergy staff were properly identifying,
No findings were identified.  
  characterizing, and correcting problems associated with this issue and whether the
4. OTHER ACTIVITIES
  planned or completed corrective actions were appropriate. The inspectors compared the
  4OA1 Performance Indicator Verification (71151 - 6 samples)
  actions taken to Entergys CAP, operability determination process, and the requirements
  of 10 CFR 50, Appendix B. The inspectors observed portions of baffle bolt replacement
Initiating Events Performance Indicators
  activities at Unit 2 and reviewed the final visual examination of the baffle bolts and plates
a. Inspection Scope
  once the work was completed.
The inspectors reviewed Entergy's submittals for the following Initiating Events
b. Findings and Observations
cornerstone performance indicators for the period April 1, 2015, to March 31, 2016:
  One Green NCV was identified and documented in Section 1R15 of this report.
Unit 2  Unplanned scrams per 7000 critical hours (IE01) Unplanned power changes per 7000 critical hours (IE03)  Unplanned scrams with complications (IE04)
  The NRC responded to the initial discovery of an unexpected number of baffle bolts
Unit 3  Unplanned scrams (IE01)  Unplanned power changes (IE03)  Unplanned scrams with complications (IE04)
  found degraded at Indian Point Unit 2 by implementing a comprehensive inspection plan
To determine the accuracy of the performance indicator data reported during those
  consisting of various baseline inspection samples to assess the extent of the issue and
periods, inspectors used definitions and guidance contained in Nuclear Energy
  to determine the necessary NRC actions. A follow-up inservice inspection sample
Institute 99-02, "Regulatory Assessment Performance Indicator Guideline," Revision 7.
  (Refer to Section 1R08) was conducted to review the capability of the non-destructive
The inspectors reviewed Entergy's operator narrative logs, maintenance planning schedules, CRs, event reports, and NRC integrated inspection reports to validate the
  examination techniques, evaluate the UT results, and observe a portion of bolt
28  accuracy of the submittals.  There were no unplanned power changes or scrams with complications during the review period.  
  replacement activities on-site. A permanent modification sample (Refer to Section
b. Findings
  1R18) was conducted to review the design change package and evaluations associated
No findings were identified.
  with the new, replacement baffle bolts. The NRC resident inspectors reviewed Entergys
  foreign material controls and loose parts analysis (Refer to Section 1R20) to address the
4OA2 Problem Identification and Resolution (71152 - 4 samples)  
  potential for missing bolt heads and concluded it would not impact safe operation of the
.1 Routine Review of Problem Identification and Resolution Activities
  plant.
a. Inspection Scope
  NRC Region I based inspectors accompanied by an expert from the NRC Office of
As required by Inspection Procedure 71152, "Problem Identification and Resolution," the  
  Nuclear Reactor Regulation completed an annual problem identification and resolution
inspectors routinely reviewed issues during baseline inspection activities and plant status reviews to verify that Entergy entered issues into the CAP at an appropriate
  inspection, documented in this section of the report, to verify that Entergys evaluations
threshold, gave adequate attention to timely corrective actions, and identified and
  and corrective actions to replace Unit 2 baffle bolts were completed in accordance with
addressed adverse trends.  In order to assist with the identification of repetitive
  an NRC approved methodology to support a conclusion that the Unit 2 baffle assembly
equipment failures and specific human performance issues for follow up, the inspectors performed a daily screening of items entered into the CAP and periodically attended CR screening meetings. The inspectors also confirmed, on a sampling basis, that, as
  meets the plant design basis. The inspectors also determined the adequacy of
applicable, for identified defects and non-conformances, Entergy performed an
  Entergys evaluations completed to determine there is a reasonable expectation that the


evaluation in accordance with 10 CFR 21.
                                          33
 
Unit 3 baffle assembly will perform as intended during the current operating cycle. The
b. Findings 
results of this review are discussed herein and in Section 1R15 of this report.
No findings were identified.
Entergy staff determined the cause of the degraded baffle bolts was primarily due to
IASCC in combination with increased fatigue loading on the baffle plates. This cause
.2 Semi-Annual Trend Review
determination was based on industry operating experience related to baffle-former bolt
a. Inspection Scope
failure in both foreign and domestic plants. IASCC is a cracking mechanism that occurs
The inspectors performed a semi-annual review of site issues, as required by Inspection
over a long period of time when susceptible metals are exposed to neutron radiation
Procedure 71152, "Problem Identification and Resolution," to identify trends that might
from the reactor core and stresses as part of normal design and operation. Entergy staff
indicate the existence of more significant safety issues.  In this review, the inspectors
concluded that failure of a critical number of bolts in a localized area subsequently
included repetitive or closely-related issues that may have been documented by Entergy outside of the CAP, such as trend reports, performance indicators, major equipment problem lists, system health reports, maintenance rule assessments, and maintenance or CAP backlogs.  The inspectors also reviewed Entergy's CAP database for the first
imposed increased loading on adjacent bolts, which propagated failures and generated
and second quarters of 2016 to assess CRs written in various subject areas (equipment
the moderate clustered pattern observed in the examination results. No other
problems, human performance issues, etc.), as well as individual issues identified during the NRCs daily CR review (Section 4OA2.1).  The inspectors reviewed the Entergy quarterly trend report for the first quarter of 2016 to verify that Entergy was appropriately
contributing causes were identified.
evaluating and trending adverse conditions in accordance with applicable procedures.
The inspectors reviewed Entergys root cause evaluation and the supporting operating
 
experience related to baffle bolt failures at other plants. The inspectors determined that
b. Findings and Observations
there is documented evidence in the existing technical literature (including materials
No findings were identified.
testing of bolts from other plants) and operating experience to conclude that the likely
cause is IASCC; however, the inspectors found that Entergy staff did not define the
The inspectors identified a trend in work being performed that was contrary to written
cause of the fatigue failure mechanism. The inspectors noted that Entergy staff sent a
work instructions and procedures, and work packages had been closed out without 
sample of baffle bolts removed from the reactor pressure vessel to a metallurgical
29  documenting the deviation from the work order.  While reviewing completed work order WO 447966 Task 10, Internal Coating Repair for 21 CCW HX, the inspectors found a
laboratory for detailed failure analysis and materials property testing. Entergy indicated
note in the work order stating that the internal coating repair to the pipe had not been done in accordance with the engineering change.  The engineering change had been written when the coating repair was expected to be small, but the actual area that was
their plans to use the results of the laboratory testing to confirm the likely root cause.
recoated was much larger.  A larger area of coating increases the impact on the heat
The inspectors concluded that Entergy staff conducted an appropriate review to identify
exchanger if the coating were to flake off and block the flow of service water.  The work
the likely causes of the degraded baffle bolts and noted that further test results will be
package was closed and no condition report was written. This performance deficiency is
used to confirm these causes.
minor because the coating was applied with procedurally directed quality controls and the likelihood that it would flake off is very small; and is the same as the original smaller area specified in the work package.  However, the work package was closed without
Following identification of the degraded baffle bolts on Unit 2, Entergys immediate
 
corrective action was to analyze the as-found condition and begin replacing bolts that
documenting the deviation and no CR was written. 
either had visual indications of bolt failure (protruding bolt head for example), did not
 
pass UT examination, or were not accessible for UT examination. The as-found number
and pattern of these bolts exceeded the acceptance criteria in the plants analysis that
In another example, the inspectors noted that WO 412920 Task 15 to perform a surge test on 11 centrifugal air compressor (CENTAC) after overhaul was completed on December 22, 2015.  However, the completion notes and documentation for the task
was prepared in advance of the baffle bolt examinations; therefore, Entergy reported this
showed that the test was unable to be performed due to a test equipment problem.  The
discovery to the NRC as an unanalyzed condition. Entergy staff completed corrective
work package was closed and no CR was written.  Subsequently, after being returned to
actions to replace all of the 227 potentially degraded baffle bolts, plus an additional 51
service, the compressor failed in service due to multiple surging events on January 7, 2016.  Troubleshooting under WO 433939 revealed that the motor high load limit had not been adjusted to account for the increased load due to reduced compressor clearances
bolts for increased structural integrity, for a total of 278 bolts. The inspectors noted the
introduced by the overhaul.  This performance deficiency is screened to minor because
51 additional bolts were installed in strategic locations to prevent clustering of potential
the 11 CENTAC is not a safety-related piece of equipment and would not affect the MC
bolt failures during the next operating cycle.
0609 cornerstone thresholds or other generic criteria.  Unit 2 and Unit 3 have dedicated
The inspectors determined that Entergy staff performed an acceptable bolt pattern
instrument air compressors that are credited in the FSAR to respond to a loss of instrument air event.  If the 11 CENTAC (located in Unit 1) were to fail, the unit-specific IACs would automatically start to prevent a loss of instrument air at both Units 2 and 3. 
analysis that evaluated the replacement bolt pattern for Unit 2 and modeled the potential
 
for future bolt failures. The inspectors found the results of the analysis accounted for a
conservative failure rate of bolts and provided appropriate margin for one cycle of
A third recent example of work being performed contrary to written instructions occurred
operation. The inspectors verified that Entergys methodology for its acceptable bolt
during 2RFO22 when the inspectors identified that the workers deviated from the surveillance procedure by demonstrating the installation of the emergency containment hatch plug without properly inflating the plug seals as directed by the procedure. This
performance deficiency was previously documented in a prior inspection report as non-cited violation 05000247/05000286/2016001-02, "Failure to Adequately Implement Risk
Management Actions for the Containment Key Safety Function."   
 
In all cases, the deviations from written work instructions were directed by Entergy supervision.  In addition, the inspectors noted that Entergy had self-identified similar
observations where work packages or condition reports had been closed without fully
completing the specified actions including CR-IP2-2015-05833, CR-IP2-2016-00103,
CR-IP3-2015-04729, CR-IP3-2016-00072, CR-IP3-2016-00075, and CR-IP3-2015-04019.  These CRs are further examples of work orders that were closed with deviations that were not documented or resolved.  Nuclear Oversight had identified several of these
condition reports.  Entergy has taking immediate corrective action in response to these
performance deficiencies. 
 
30  .3 Annual Sample:  Maintenance Rule Self-Assessment of Corrective Actions
a. Inspection Scope
The inspectors performed an in-depth review of Entergy's corrective actions associated
with self-assessment LO-IP3LO-2015-72, "Maintenance Rule (a)(3) Assessment."  The self-assessment was performed to satisfy both the self-assessment criteria in EN-LI-104,
"Self-Assessment and Benchmark Process," and the maintenance rule periodic
assessment criteria in EN-DC-207. 
The inspectors assessed Entergy's problem identification threshold, extent of condition
reviews, and the prioritization and timeliness of Entergy corrective actions to determine
whether Entergy was appropriately identifying, characterizing, and correcting problems
associated with this issue and whether the planned or completed corrective actions were appropriate.  The inspectors compared the actions taken to the requirements of Entergy's CAP and 10 CFR 50, Appendix B.  In addition, the inspectors interviewed
engineering personnel to assess the effe
ctiveness of the im
plemented corrective actions. 
 
b. Findings and Observations
No findings were identified. 
 
Entergy identified three standard deficiencies during their self-assessment and wrote
CRs to document each one.  One of the standard deficiencies was that the maintenance rule basis documents were not being reviewed at least once every two years as required by procedure EN-DC-204, "Maintenance Rule Scope and Basis."  The purpose of this
review was to ensure that the documents were updated if the configuration of the system
changed or if the performance criteria needed to be adjusted.  Entergy wrote CR-IP3-
2015-03628 and assigned a corrective action to create work trackers to perform the basis document reviews.  They chose to use work trackers instead of corrective actions under the CAP because the work had historically been assigned using work trackers. 
However, because work trackers do not receive the same priority as corrective actions,
some of the maintenance rule basis documents had still not been reviewed at the time of
this inspection, over a year after the completion of the self-assessment.  The inspectors
determined that this was not a more than minor issue because the systems in question did not show signs of inadequate maintenance.
.4 Annual Sample:  Unit 2 Reactor Trip on December 5, 2015
a. Inspection Scope
The inspectors performed an in-depth review of Entergy's evaluations and corrective
actions associated with
CR-IP2-2015-05484
and the related apparent cause evaluation for the December 5, 2015, manual reactor trip in response to indications of multiple
dropped control rods caused by the loss of control rod power due to a power supply
failure.  Entergy performed an apparent cause evaluation and determined the
direct cause of the event was the loss of motor control center (MCC)-24 due to an internal fault at the line side leads at cubicle 2H where they connect to the bucket stab assemblies. 
The apparent cause was an unanticipated loss of power to the control rod system due to
the degradation of the primary control rod power supply (PS1) which failed to function for 
31  more than 10 minutes when the operating alternate power supply (PS2) was deenergized. 
 
The inspectors assessed Entergy's problem identification threshold, problem analysis, extent of condition reviews, compensatory actions, and the prioritization and timeliness
of Entergy's corrective actions to determine whether Entergy was appropriately
identifying, characterizing, and correcting problems associated with this issue and
whether the planned or completed corrective actions were appropriate.  The inspectors
compared the actions taken to the requirements of Entergy's CAP and 10 CFR 50, Appendix B, Criterion XVI, "Corrective Action." 
b. Findings and Observations
No findings were identified. 
The inspectors found that Entergy took appropriate actions to identify the direct and
apparent cause of the issue.  The
direct cause of the event was the loss of MCC-24 due to an internal fault at the line side leads at cubicle 2H where they connect to the bucket
stab assemblies.  The apparent cause was an unanticipated loss of power to the control rod system due to the degradation of the primary control rod PS1, which failed to function when PS2 was lost.  Entergy replaced the degraded rod control PS1; and the
MCC-24 compartments were removed to facilitate inspection and testing of the MCC
bus, control wires, and MCC internal.  PS2 was also restored to operation after the fault
was cleared. 
The inspector determined that the internal electrical fault that deenergized PS2 and the prior degradation in PS1 was not within Entergy's ability to foresee and prevent. 
Therefore, there was no performance deficiency identified.  Entergy's overall response to
the issue was commensurate with the safety significance, was timely, and the actions
taken and planned were reasonable to resolve the failure of the primary control rod PS1.
.5 Annual Sample:  Unexpected Number of Degraded Baffle-Former Bolts Discovered in
the Unit 2 Reactor Pressure Vessel
a. Inspection Scope
The inspectors performed an in-depth review of Entergy's root cause evaluation and corrective actions associated with CR-IP2-2016-02348 for baffle-former ("baffle") bolts
found with indications of degradation during the Indian Point Unit 2 RFO 2R22.  Entergy
performed ultrasonic examinations of the baffle bolts in accordance with their procedures
as part of a planned activity.  After an unexpected number of degraded baffle bolts were discovered, Entergy staff reported the issue to the NRC as Event Notification No. 51829 on March 29, 2016, because the as-found number and location of degraded bolts
represented an unanalyzed condition.  Entergy staff completed corrective actions to
replace all of the potentially degraded baffle bolts on Unit 2.  Entergy staff further
replaced a population of additional bolts that exhibited no indications of degradation and
performed an evaluation to determine the potential for baffle bolt failures at Unit 3.
The baffle-former bolts help secure vertical plates (also referred to as baffle plates)
inside the reactor vessel, which then forms a structure surrounding the reactor fuel
assemblies to orient the fuel and to direct coolant flow through the core.  A sufficient 
32  number of baffle bolts are required to remain intact to secure the baffle plates in place so as to not affect control rod insertion or impede emergency core cooling flow during
postulated accident conditions.  Bolt heads that separate and are no longer held in place by bolt lock-tabs can also become a loose parts concern.
The inspectors determined whether Entergy's acceptable baffle bolt pattern analysis for
Unit 2 was completed in accordance with the NRC-approved methodology and provided
appropriate structural margin for the next cycle of operation to ensure the Unit 2 baffle
plates will remain in place during both normal operation and limiting postulated accident conditions.  The inspectors further determined whether Entergy's evaluations of the baffle bolts installed in Indian Point Unit 3 were technically sufficient to conclude the
Unit 3 baffle assembly will perform as intended until the next planned RFO, at which time
Entergy plans to examine the bolts.  The inspectors reviewed Entergy's procedures for
determining the functionality and operability of degraded SSC as they relate to Unit 3.  The inspectors further interviewed Entergy engineering personnel and contractor staff to discuss the results of Entergy's technical evaluations and to assess the effectiveness of
the implemented and planned corrective actions.
 
The inspectors assessed Entergy's problem identification threshold, cause analyses, extent of condition, compensatory actions, and the prioritization and timeliness of Entergy's corrective actions to determine whether Entergy staff were properly identifying,
characterizing, and correcting problems associated with this issue and whether the
planned or completed corrective actions were appropriate.  The inspectors compared the
actions taken to Entergy's CAP, operability determination process, and the requirements
of 10 CFR 50, Appendix B.  The inspectors observed portions of baffle bolt replacement activities at Unit 2 and reviewed the final visual examination of the baffle bolts and plates once the work was completed.
b. Findings and Observations
One Green NCV was identified and documented in Section 1R15 of this report. The NRC responded to the initial discovery of an unexpected number of baffle bolts
found degraded at Indian Point Unit 2 by implementing a comprehensive inspection plan
consisting of various baseline inspection samples to assess the extent of the issue and
to determine the necessary NRC actions.  A follow-up inservice inspection sample
(Refer to Section 1R08) was conducted to review the capability of the non-destructive examination techniques, evaluate the UT results, and observe a portion of bolt replacement activities on-site.  A permanent modification sample (Refer to Section
1R18) was conducted to review the design change package and evaluations associated
 
with the new, replacement baffle bolts.  The NRC resident inspectors reviewed Entergy's
foreign material controls and loose parts analysis (Refer to Section 1R20) to address the potential for missing bolt heads and concluded it would not impact safe operation of the
plant.
NRC Region I based inspectors accompanied by an expert from the NRC Office of Nuclear Reactor Regulation completed an annual problem identification and resolution
inspection, documented in this section of the report, to verify that Entergy's evaluations and corrective actions to replace Unit 2 baffle bolts were completed in accordance with an NRC approved methodology to support a conclusion that the Unit 2 baffle assembly
meets the plant design basis.  The inspectors also determined the adequacy of
Entergy's evaluations completed to determine there is a reasonable expectation that the 
33  Unit 3 baffle assembly will perform as intended during the current operating cycle. The results of this review are discussed herein and in Section 1R15 of this report.  
 
Entergy staff determined the cause of the degraded baffle bolts was primarily due to IASCC in combination with increased fatigue loading on the baffle plates. This cause  
determination was based on industry operating experience related to baffle-former bolt  
failure in both foreign and domestic plants. IASCC is a cracking mechanism that occurs  
over a long period of time when susceptible metals are exposed to neutron radiation  
from the reactor core and stresses as part of normal design and operation. Entergy staff concluded that failure of a critical number of bolts in a localized area subsequently imposed increased loading on adjacent bolts, which propagated failures and generated  
the moderate clustered pattern observed in the examination results. No other  
contributing causes were identified.  
 
The inspectors reviewed Entergy's root cause evaluation and the supporting operating experience related to baffle bolt failures at other plants. The inspectors determined that  
there is documented evidence in the existing technical literature (including materials  
testing of bolts from other plants) and operating experience to conclude that the likely  
cause is IASCC; however, the inspectors found that Entergy staff did not define the cause of the fatigue failure mechanism. The inspectors noted that Entergy staff sent a sample of baffle bolts removed from the reactor pressure vessel to a metallurgical  
laboratory for detailed failure analysis and materials property testing. Entergy indicated  
their plans to use the results of the laboratory testing to confirm the likely root cause.
The inspectors concluded that Entergy staff conducted an appropriate review to identify  
the likely causes of the degraded baffle bolts and noted that further test results will be used to confirm these causes.  
Following identification of the degraded baffle bolts on Unit 2, Entergy's immediate  
corrective action was to analyze the as-found condition and begin replacing bolts that  
either had visual indications of bolt failure (protruding bolt head for example), did not pass UT examination, or were not accessible for UT examination. The as-found number and pattern of these bolts exceeded the acceptance criteria in the plant's analysis that  
was prepared in advance of the baffle bolt examinations; therefore, Entergy reported this  
discovery to the NRC as an unanalyzed condition. Entergy staff completed corrective  
actions to replace all of the 227 potentially degraded baffle bolts, plus an additional 51  
bolts for increased structural integrity, for a total of 278 bolts. The inspectors noted the 51 additional bolts were installed in strategic locations to prevent clustering of potential bolt failures during the next operating cycle.  
 
The inspectors determined that Entergy staff performed an acceptable bolt pattern  
analysis that evaluated the replacement bolt pattern for Unit 2 and modeled the potential for future bolt failures. The inspectors found the results of the analysis accounted for a conservative failure rate of bolts and provided appropriate margin for one cycle of  
operation. The inspectors verified that Entergy's methodology for its acceptable bolt  
pattern analyses, including its determination of margin, was consistent with the NRC-
pattern analyses, including its determination of margin, was consistent with the NRC-
approved methodology in topical report WCAP-15029-NP-A (ML15222A882). The  
approved methodology in topical report WCAP-15029-NP-A (ML15222A882). The
inspectors determined that Entergy staff tracked corrective actions to re-examine the Unit 2 baffle bolts during the next planned RFO. The inspectors noted the new baffle bolts were made of a material with improved resistance to IASCC and included an  
inspectors determined that Entergy staff tracked corrective actions to re-examine the
improved design to reduce the stresses at the head to shank transition, both of which  
Unit 2 baffle bolts during the next planned RFO. The inspectors noted the new baffle
are enhancements compared to the original bolts.
bolts were made of a material with improved resistance to IASCC and included an
34  As part of an extent of condition assessment, Entergy entered CR-IP3-2016-01035 in its CAP to evaluate the potential for degraded baffle bolts on Unit 3.  Entergy operators
improved design to reduce the stresses at the head to shank transition, both of which
performed an IOD and concluded that the baffle assembly was operable.  Entergy staff performed a subsequent "extent of condition review" that concluded Unit 3 would experience less baffle bolt degradation than Unit 2 based on several plant factors. 
are enhancements compared to the original bolts.
Entergy also conducted sensitivity analyses to show acceptable bounding conditions in
the event of bolt failures.  The inspectors reviewed Entergy's evaluations and noted that
Entergy staff concluded there was not a degraded condition at Unit 3.  In consideration
of the guidance in their operability procedure and operating experience from Unit 2 and other plants, the NRC issued an NCV in this report because Entergy did not perform an operability evaluation for Unit 3 as a follow-up to the immediate determination for the
potential impact on supported systems controlled by the TS (Refer to Section 1R15).
As a corrective action, Entergy staff performed an operability evaluation and demonstrated that the Unit 3 baffle former assembly remained operable.  The inspectors concluded that this supplemental evaluation provided appropriate technical justification
for the continued operation of Unit 3 until the next RFO in spring 2017, at which time
Entergy plans to examine the baffle bolts.  Entergy also implemented a corrective action
as part of an enhancement to plant operations to monitor the RCS for any signs of fuel leakage, which could be an indicator of baffle bolt failures. 
The inspectors reviewed Westinghouse Nuclear Safety Advisory Letter NSAL-16-1,
which discussed the results of recent baffle-former bolt inspections and provided
Westinghouse's recommendations on this issue.  The letter described the plants as most
susceptible (i.e. Tier 1a) to this degradation as Westinghouse 4-loop reactors limited to those with a down-flow configuration and using Type 347 stainless steel bolts.  The inspectors noted the recommendation was to complete UT volumetric examination of the
baffle bolts at the next scheduled RFO, and that Entergy had already planned this action
for Unit 3.  Entergy also planned a long-term corrective action to convert Units 2 and 3
from a "down-flow" baffle configuration to an "up-flow" configuration, which would
significantly reduce the load on baffle-former bolts and provide for increased structural margin of the baffle-former assembly.  The inspectors determined Entergy's overall
response to the issue was commensurate with the safety significance, was timely, and
included appropriate compensatory actions.  The inspectors concluded that the actions
completed and planned were reasonable to address the ongoing aging management of
baffle bolts.
4OA3 Follow Up of Events and Notices of Enforcement Discretion (71153 - 5 samples)
.1 Plant Events
a. Inspection Scope
For the plant events listed below, the inspectors reviewed and/or observed plant
parameters, reviewed personnel performance, and evaluated performance of mitigating
systems.  The inspectors communicated the plant events to appropriate regional
personnel, and compared the event details with criteria contained in IMC 0309, "Reactive Inspection Decision Basis for Reactors," for consideration of potential reactive inspection activities.  As applicable, the inspectors verified that Entergy made appropriate
emergency classification assessments and properly reported the event in accordance with 10 CFR 50.72 and 50.73.  The inspectors reviewed Entergy's follow-up actions 
35  related to the events to assure that Entergy implemented appropriate corrective actions commensurate with their safety significance. 
 
Unit 2  Turbine trip occurred while synchronizing Unit 2 to the grid on June 15, 2016  Shutdown required by TS for repairs to a leak on the 21 CCW heat exchanger  service water inlet on June 23, 2016
Unit 3  Rapid power reduction from 100 percent to 45 percent power in response to a loss of both heater drain pumps on May 26, 2016
b. Findings
No findings were identified.
.2 (Closed) Licensee Event Report (LER) 05000247/2015-003-00:  Manual Reactor Trip Due to Indications of Multiple Dropped Control Rods Caused by Loss of Control Rod Power Due to a Power Supply Failure
The inspector's reviewed Entergy's actions and reportability criteria associated with LER
05000247/2015-003-00, which was submitted to the NRC on February 3, 2016.  On
December 5, 2015, control room operators initiated a manual reactor trip after observing indications consistent with multiple dropped control rods following an alarm for the trip of MCC-24/24A.  No control rod indication was available due to MCC-24 being faulted and
de-energized.  The
direct cause of the event was the loss of MCC-24 due to an internal fault at the line sides leads at cubicle 2H where they connect to the bucket stab
assemblies.  The apparent cause was an unanticipated loss of power to the control rod
system due to the degradation of the primary control rod PS1 which failed to function when the operating PS2 was lost.  The inspectors determined that both the unexpected failure of PS2 and the internal fault in PS1 was not within Entergy's ability to foresee and
prevent and was not a performance deficiency.  The inspectors reviewed the LER, the
associated apparent cause evaluation analysis, and interviewed Entergy staff.  This LER is closed.
.3 (Closed) LER 05000247/2016-003-00:  TS Prohibited Condition Due to an Inoperable 21 MBFP Discharge Valve for Greater Than the TS Allowed Outage Time
 
The inspector's reviewed Entergy's actions and reportability criteria associated with LER 05000247/2016-003-00, which was submitted to the NRC on May 6, 2016.  On March 7, 2016, during the shutdown to enter 2RFO22, the control switch for the 21 MBFP was
tripped from the control room but the MBFP discharge valve BFD-2-21 failed to fully
close as designed.  The MBFP discharge valve was declared inoperable and TS 3.7.3
Condition C was entered.  The MFD-2-21 isolation valve was then manually closed.  The
direct cause of the failure to close the MBFP discharge valve BFD-2-21 was the motor operated valve's (MOV's) close torque switch contact finger out of position.  The apparent cause was that the MOV preventative maintenance procedure lacked the level
of detail and direction due to an unrecognized susceptibility associated with the
orientation of the close torque switch contact finger bracket opening and spreading of 
36  the "U" shape bracket.  The downward arrangement made it easier for the torque switch contact finger to move out with spreading of the "U" shaped contact holder.  The
inspectors reviewed the LER, the associated apparent cause evaluation analysis, and interviewed Entergy staff.  This LER is closed. 
Introduction.  The inspectors identified a Green NCV of 10 CFR 50.65(b)(1) for Entergy's failure to include a function of a safety-related system within the scope of the
maintenance rule program.  Specifically, Entergy failed to include the feedwater isolation
function performed by the MBFP discharge valves, MBFPs, and feedwater regulating
valves and feedwater isolation valves which are required to remain functional during and following a design basis event to mitigate the consequences of an accident, within the
scope of the maintenance rule monitoring program. 
  Description.  On March 7, 2016, during an RFO, the control switch for the 21 MBFP was positioned to trip and the 21 MBFP tripped as designed, but the MBFP discharge valve
BFD-2-21 failed to fully close.  Entergy declared MBFP discharge valve BFD-2-21
inoperable and entered TS 3.7.3 Condition C.  After troubleshooting, Entergy determined
the MOV close torque switch contact finger was out of position within the contact holder. 
The misalignment allowed the contact finger to move out of the proper position causing the MOV BFD-2-21 to fail to close.  This is the same failure mechanism which caused MOV BFD-2-21 to fail to close in 2010 which is referenced in CR-IP2-2010-07013.  On
December 5, 2015, the 21 MBFP failed to trip and required closure of the steam
admission valves to secure it.  This failure occurred because of contaminated control oil
that prevented the solenoid valves from operating. 
The inspectors reviewed Entergy's maintenance rule basis documents and identified the feedwater isolation function was not properly included in the maintenance rule
monitoring program as required by 10 CFR 50.65(b)(1).  The basis document for the
feedwater system did identify the need to monitor the feedwater isolation function under
the maintenance rule and stated that it would be monitored as a part of the vapor containment supersystem.  However, the basis document for the vapor containment supersystem does not include the feedwater isolation components within the system boundaries.  As a result, when component failures occurred which affected the
feedwater isolation function, they were not reviewed to determine if they were
 
maintenance rule functional failures; and Entergy was unable to identify that the
performance of the main feedwater isolation equipment was not effectively controlled through preventative maintenance.  Entergy entered this issue into the CAP as CR-IP2-2016-03963 and initiated actions to include the MBFP discharge valves into the
maintenance rule program. 
 
Analysis.  The failure to appropriately scope the safety-related feedwater isolation function within the maintenance rule program was a performance deficiency.  This
finding is more than minor because it is associated with the SSC and barrier
performance attribute of the Barrier Integrity cornerstone and affected the cornerstone
objective to provide reasonable assurance that physical design barriers protect the
public from radionuclide releases caused by acci
dents or events.  Specifically, the failure to properly scope the feedwater isolation function prevented Entergy from identifying that equipment reliability was no longer effectively controlled through preventative maintenance.  Additionally, this issue is similar to example 7.d described in IMC 0612, Appendix E, "Examples of Minor Issues," dated August 11, 2009.  In accordance with
IMC 0609.04, "Initial Characterization of Findings," and Exhibit 2 of IMC 0609, Appendix 
37  A, "The Significance Determination Process for Findings At-Power," issued June 19, 2012, the inspectors determined that the finding was of very low safety significance
(Green) because the finding did not represent an actual open pathway in the physical integrity of reactor containment, containment isolation system, and heat removal components.  There are redundant methods of feedwater isolation.  They include
tripping the MBFPs and closing the MBFP discharge valves, closing the main feedwater
regulating valves and low flow bypass valves, and closing the main feedwater isolation
valves.  On both December 5, 2015, and March 7, 2016, the main feedwater regulating
valves and isolation valves were functional; so there was no loss of the ability to isolate feedwater to mitigate accident and transient conditions. 
This finding does not have a cross-cutting aspect, since the failure to scope this
equipment into the maintenance rule program was not recognized when Entergy
combined the maintenance rule basis documents for Units 2 and 3 in 2012 and as a result, is not indicative of current licensee performance. 
Enforcement.
  10 CFR 50.65(b)(1) requires, in part, that the holders of an operating license shall include within the scope of the monitoring program, specified in 10 CFR 50.65(a)(1), SSCs that are relied upon to remain functional during and following
design basis events.  Contrary to the
above, since the combined maintenance rule scoping for Units 2 and 3 in 2012, Entergy failed to include within the scope of the
monitoring program specified in 10 CFR 50.65(a)(1), the safety-related MBFP discharge
valves.  These SSCs are relied upon during and after design basis events to mitigate the
consequences of a feedwater line break accident inside containment.  Entergy's
corrective action included entering this issue into the corrective action program.  Because the violation was of very low safety significance (Green) and Entergy entered this issue into their CAP as CR-IP2-2016-03963, this violation is being treated as an
NCV, consistent with Section 2.3.2.a of the NRC Enforcement Policy.  (NCV 05000247/2016002-04, Failure to Scope Safety-Related Main Boiler Feedwater Pump Discharge Valves into the Maintenance Rule Program)
  4OA5 Other Activities
.1 Groundwater Contamination
a. Inspection Scope
On February 5, 2016, Entergy notified the NRC of a significant increase in groundwater
 
tritium levels measured at three monitoring wells (MWs) (MW-30, MW-31, and MW-32) located near the Unit 2 fuel storage building.  These samples were drawn on
January 26 to 27, 2016, and analyzed and confirmed on February 2 to 4, 2016.  The highest concentration was detected at MW-32, which increased from 12,000 pCi/l on January 11, 2016, to 8,100,000 pCi/l on January 26, 2016, and subsequently up to
14,800,000 pCi/l on February 4, 2016.  This increased tritium concentration event was
documented by Entergy in CR-IP2-2016-00564 which documents its investigation of this
event including a root cause evaluation.  The inspectors reviewed Entergy's root cause evaluation for this event during this inspection period as well as recent groundwater monitoring results.
   
38  b. Findings and Observations
  No findings were identified.
Update to URI 05000247/2016001-07, January 2016 Groundwater Contamination
Entergy continues to conduct weekly, biweekly, and monthly groundwater sampling of
MWs at the initial site of groundwater contamination and at downstream wells towards
the Hudson River.  For the initial three MWs (MW-30, MW-31, and MW-32), the general trend in tritium activity has been downward, with periodic increases seen in some weekly samples.  The downstream MWs located in the Unit 2 switchyard (especially MW-55)
showed an initial increase in activity up to 117,000 pCi/l, but the activity at that location
has plateaued at the end of the reporting period.
Entergy documented its investigation of this event as root cause evaluation for CR-IP2-2016-00564.  The inspectors reviewed Entergy's root cause evaluation for this
event.  Entergy concluded that the source of the groundwater contamination was from the reject water of a temporary reverse osmosis unit used to process water from the
refueling water storage tank at Unit 2 in preparation for RFO 2R22.  Although this analysis documents a number of issues identified during the operation of the contractor reverse osmosis unit, which is believed to be the source of the groundwater
contamination, one of two leakage paths to groundwater have still not been established. 
The established pathway involves leakage from two cut drain lines located above the floor on the 35-foot elevation of the PAB.  Further investigation by Entergy following the
conclusion of the Unit 2 RFO 2R22 must be conducted to verify the second pathway to
groundwater via the floor of the fuel storage building truck bay.
Entergy's long-term corrective action for reducing tritium levels in the groundwater is the
same as previously identified for the March 2014 tritium spike (CR-IP2-2015-03806), the
start-up and operation of recovery well (RW)-1.  Following installation of equipment and system testing, full operation of the RW system is expected later this year.  This system will allow for the collection of tritiated groundwater in the vicinity of Unit 2 to be returned
inside the Unit 2 PAB for processing.  The NRC will be conducting an inspection in
 
August 2016 to review the testing plan and results of the RW-1 tests.  This inspection
will include a specialist region-based inspector, and a staff hydrogeologist.
 
The NRC's continuing assessment of the safety
significance of this event focused on validating the safety impact of dose to the public from the release of tritium to the site
groundwater, and ultimately to the Hudson River.  The NRC verified that Entergy's
bounding public dose calculations on the groundwater contamination leak was
sufficiently conservative and a maximum worst case scenario would result in a dose of
0.000112 millirem per year, which represents a very small fraction of the allowable dose (liquid effluent dose objective of 3 millirem per year).  This low value is due to
groundwater at Indian Point not being a source of any drinking water.  There are no
drinking water wells on the Indian Point site, groundwater flow from the site is to the
Hudson River and not to any near site drinking water wells, and the Hudson River has
no downstream drinking water intakes as it is brackish water.  Pathways to the public are therefore limited to the consumption of fish and river invertebrates.  The inspection determined that there is no safety impact to the public as a result of this groundwater
 
contamination event.  (URI 05000247/2016001-07, January 2016 Groundwater
Contamination)
 
39    .2 Institute of Nuclear Power Operations (INPO) Report Review
a. Inspection Scope
The inspectors also reviewed the final report for the INPO equipment reliability scram
review visit that was conducted to review the scrams that occurred over the past two
years, conducted in June 2016.  The inspectors reviewed the report to ensure that any
issues identified were consistent with NRC perspectives of Entergy performance and to determine if INPO identified any significant safety issues that required further NRC
follow-up.
 
b. Findings
No findings were identified.
4OA6 Meetings, Including Exit
On August 4, 2016, the inspectors presented the inspection results to Mr. Larry Coyle, Site Vice President, and other members of Entergy.  Based on additional information provided, the inspectors conducted an updated exit meeting on August 30, 2016 with
John Kirkpatrick, Plant Operations General Manager and other members of Entergy. 
The inspectors verified that no proprietary information was retained by the inspectors or
documented in this report.
  ATTACHMENT:  SUPPLEMENTARY INFORMATION
 
A-1  Attachment SUPPLEMENTARY INFORMATION
KEY POINTS OF CONTACT
  Entergy Personnel
A. Vitale, Site Vice President


J. Kirkpatrick, Plant Operations General Manager
                                                34
R. Alexander, Unit 2 Shift Manager
      As part of an extent of condition assessment, Entergy entered CR-IP3-2016-01035 in its
R. Andersen, Maintenance Instrumentation and Controls Superintendent N. Azevedo, Engineering Supervisor 
      CAP to evaluate the potential for degraded baffle bolts on Unit 3. Entergy operators
J. Baker, Shift Manager
      performed an IOD and concluded that the baffle assembly was operable. Entergy staff
      performed a subsequent extent of condition review that concluded Unit 3 would
      experience less baffle bolt degradation than Unit 2 based on several plant factors.
      Entergy also conducted sensitivity analyses to show acceptable bounding conditions in
      the event of bolt failures. The inspectors reviewed Entergys evaluations and noted that
      Entergy staff concluded there was not a degraded condition at Unit 3. In consideration
      of the guidance in their operability procedure and operating experience from Unit 2 and
      other plants, the NRC issued an NCV in this report because Entergy did not perform an
      operability evaluation for Unit 3 as a follow-up to the immediate determination for the
      potential impact on supported systems controlled by the TS (Refer to Section 1R15).
      As a corrective action, Entergy staff performed an operability evaluation and
      demonstrated that the Unit 3 baffle former assembly remained operable. The inspectors
      concluded that this supplemental evaluation provided appropriate technical justification
      for the continued operation of Unit 3 until the next RFO in spring 2017, at which time
      Entergy plans to examine the baffle bolts. Entergy also implemented a corrective action
      as part of an enhancement to plant operations to monitor the RCS for any signs of fuel
      leakage, which could be an indicator of baffle bolt failures.
      The inspectors reviewed Westinghouse Nuclear Safety Advisory Letter NSAL-16-1,
      which discussed the results of recent baffle-former bolt inspections and provided
      Westinghouses recommendations on this issue. The letter described the plants as most
      susceptible (i.e. Tier 1a) to this degradation as Westinghouse 4-loop reactors limited to
      those with a down-flow configuration and using Type 347 stainless steel bolts. The
      inspectors noted the recommendation was to complete UT volumetric examination of the
      baffle bolts at the next scheduled RFO, and that Entergy had already planned this action
      for Unit 3. Entergy also planned a long-term corrective action to convert Units 2 and 3
      from a down-flow baffle configuration to an up-flow configuration, which would
      significantly reduce the load on baffle-former bolts and provide for increased structural
      margin of the baffle-former assembly. The inspectors determined Entergys overall
      response to the issue was commensurate with the safety significance, was timely, and
      included appropriate compensatory actions. The inspectors concluded that the actions
      completed and planned were reasonable to address the ongoing aging management of
      baffle bolts.
4OA3 Follow Up of Events and Notices of Enforcement Discretion (71153 - 5 samples)
.1    Plant Events
  a. Inspection Scope
      For the plant events listed below, the inspectors reviewed and/or observed plant
      parameters, reviewed personnel performance, and evaluated performance of mitigating
      systems. The inspectors communicated the plant events to appropriate regional
      personnel, and compared the event details with criteria contained in IMC 0309, Reactive
      Inspection Decision Basis for Reactors, for consideration of potential reactive inspection
      activities. As applicable, the inspectors verified that Entergy made appropriate
      emergency classification assessments and properly reported the event in accordance
      with 10 CFR 50.72 and 50.73. The inspectors reviewed Entergys follow-up actions


S. Bianco, Operations Fire Marshal
                                                35
K. Brooks, Assistant Operations Manager
      related to the events to assure that Entergy implemented appropriate corrective actions
R. Burroni, Engineering Director  T. Chan, Engineering Supervisor C. Chapin, Training Superintendent
      commensurate with their safety significance.
D. Dewey, Assistant Operations Manager
      Unit 2
J. Dignam, Unit 3 Control Room Supervisor
          Turbine trip occurred while synchronizing Unit 2 to the grid on June 15, 2016
R. Dolansky, Inservice Inspection Program Manager W. Durr, Outage Control Center Manager R. Drake, Engineering Supervisor
          Shutdown required by TS for repairs to a leak on the 21 CCW heat exchanger
K. Elliott, Fire Protection Engineer 
          service water inlet on June 23, 2016
J. Ferrick, Regulatory and Performance Improvement Director
      Unit 3
L. Frink, Radiation Protection Supervisor
          Rapid power reduction from 100 percent to 45 percent power in response to a loss of
D. Gagnon, Security Manager L. Glander, Emergency Preparedness Manager D. Gray, Radiological Environmental Manager
          both heater drain pumps on May 26, 2016
J. Johnson, Unit 2 Control Room Supervisor
  b. Findings
      No findings were identified.
.2    (Closed) Licensee Event Report (LER) 05000247/2015-003-00: Manual Reactor Trip
      Due to Indications of Multiple Dropped Control Rods Caused by Loss of Control Rod
      Power Due to a Power Supply Failure
      The inspectors reviewed Entergys actions and reportability criteria associated with LER
      05000247/2015-003-00, which was submitted to the NRC on February 3, 2016. On
      December 5, 2015, control room operators initiated a manual reactor trip after observing
      indications consistent with multiple dropped control rods following an alarm for the trip of
      MCC-24/24A. No control rod indication was available due to MCC-24 being faulted and
      de-energized. The direct cause of the event was the loss of MCC-24 due to an internal
      fault at the line sides leads at cubicle 2H where they connect to the bucket stab
      assemblies. The apparent cause was an unanticipated loss of power to the control rod
      system due to the degradation of the primary control rod PS1 which failed to function
      when the operating PS2 was lost. The inspectors determined that both the unexpected
      failure of PS2 and the internal fault in PS1 was not within Entergys ability to foresee and
      prevent and was not a performance deficiency. The inspectors reviewed the LER, the
      associated apparent cause evaluation analysis, and interviewed Entergy staff. This LER
      is closed.
.3    (Closed) LER 05000247/2016-003-00: TS Prohibited Condition Due to an Inoperable 21
      MBFP Discharge Valve for Greater Than the TS Allowed Outage Time
      The inspectors reviewed Entergys actions and reportability criteria associated with LER
      05000247/2016-003-00, which was submitted to the NRC on May 6, 2016. On March 7,
      2016, during the shutdown to enter 2RFO22, the control switch for the 21 MBFP was
      tripped from the control room but the MBFP discharge valve BFD-2-21 failed to fully
      close as designed. The MBFP discharge valve was declared inoperable and TS 3.7.3
      Condition C was entered. The MFD-2-21 isolation valve was then manually closed. The
      direct cause of the failure to close the MBFP discharge valve BFD-2-21 was the motor
      operated valves (MOVs) close torque switch contact finger out of position. The
      apparent cause was that the MOV preventative maintenance procedure lacked the level
      of detail and direction due to an unrecognized susceptibility associated with the
      orientation of the close torque switch contact finger bracket opening and spreading of


M. Johnson, Unit 3 Shift Manager 
                                          36
M. Khadabux, Instrumentation and Controls Supervisor F. Kich, Performance Improvement Manager M. Lewis, Unit 3 Assistant Operations Manager
the U shape bracket. The downward arrangement made it easier for the torque switch
N. Lizzo, Training Manager
contact finger to move out with spreading of the U shaped contact holder. The
S. McAllister, Baffle Bolt Replacement Project Manager
inspectors reviewed the LER, the associated apparent cause evaluation analysis, and
M. McCarthy, Unit 3 Control Room Supervisor
interviewed Entergy staff. This LER is closed.
Introduction. The inspectors identified a Green NCV of 10 CFR 50.65(b)(1) for Entergys
failure to include a function of a safety-related system within the scope of the
maintenance rule program. Specifically, Entergy failed to include the feedwater isolation
function performed by the MBFP discharge valves, MBFPs, and feedwater regulating
valves and feedwater isolation valves which are required to remain functional during and
following a design basis event to mitigate the consequences of an accident, within the
scope of the maintenance rule monitoring program.
Description. On March 7, 2016, during an RFO, the control switch for the 21 MBFP was
positioned to trip and the 21 MBFP tripped as designed, but the MBFP discharge valve
BFD-2-21 failed to fully close. Entergy declared MBFP discharge valve BFD-2-21
inoperable and entered TS 3.7.3 Condition C. After troubleshooting, Entergy determined
the MOV close torque switch contact finger was out of position within the contact holder.
The misalignment allowed the contact finger to move out of the proper position causing
the MOV BFD-2-21 to fail to close. This is the same failure mechanism which caused
MOV BFD-2-21 to fail to close in 2010 which is referenced in CR-IP2-2010-07013. On
December 5, 2015, the 21 MBFP failed to trip and required closure of the steam
admission valves to secure it. This failure occurred because of contaminated control oil
that prevented the solenoid valves from operating.
The inspectors reviewed Entergys maintenance rule basis documents and identified the
feedwater isolation function was not properly included in the maintenance rule
monitoring program as required by 10 CFR 50.65(b)(1). The basis document for the
feedwater system did identify the need to monitor the feedwater isolation function under
the maintenance rule and stated that it would be monitored as a part of the vapor
containment supersystem. However, the basis document for the vapor containment
supersystem does not include the feedwater isolation components within the system
boundaries. As a result, when component failures occurred which affected the
feedwater isolation function, they were not reviewed to determine if they were
maintenance rule functional failures; and Entergy was unable to identify that the
performance of the main feedwater isolation equipment was not effectively controlled
through preventative maintenance. Entergy entered this issue into the CAP as
CR-IP2-2016-03963 and initiated actions to include the MBFP discharge valves into the
maintenance rule program.
Analysis. The failure to appropriately scope the safety-related feedwater isolation
function within the maintenance rule program was a performance deficiency. This
finding is more than minor because it is associated with the SSC and barrier
performance attribute of the Barrier Integrity cornerstone and affected the cornerstone
objective to provide reasonable assurance that physical design barriers protect the
public from radionuclide releases caused by accidents or events. Specifically, the failure
to properly scope the feedwater isolation function prevented Entergy from identifying that
equipment reliability was no longer effectively controlled through preventative
maintenance. Additionally, this issue is similar to example 7.d described in IMC 0612,
Appendix E, Examples of Minor Issues, dated August 11, 2009. In accordance with
IMC 0609.04, Initial Characterization of Findings, and Exhibit 2 of IMC 0609, Appendix


B. McCarthy, Operations Manager F. Mitchell, Radiation Protection Manager E. Mullek, Maintenance Manager
                                                37
S. Stevens, Radiation Protection Operations Superintendent
      A, The Significance Determination Process for Findings At-Power, issued June 19,
B. Sullivan, Training Superintendent
      2012, the inspectors determined that the finding was of very low safety significance
      (Green) because the finding did not represent an actual open pathway in the physical
      integrity of reactor containment, containment isolation system, and heat removal
      components. There are redundant methods of feedwater isolation. They include
      tripping the MBFPs and closing the MBFP discharge valves, closing the main feedwater
      regulating valves and low flow bypass valves, and closing the main feedwater isolation
      valves. On both December 5, 2015, and March 7, 2016, the main feedwater regulating
      valves and isolation valves were functional; so there was no loss of the ability to isolate
      feedwater to mitigate accident and transient conditions.
      This finding does not have a cross-cutting aspect, since the failure to scope this
      equipment into the maintenance rule program was not recognized when Entergy
      combined the maintenance rule basis documents for Units 2 and 3 in 2012 and as a
      result, is not indicative of current licensee performance.
      Enforcement. 10 CFR 50.65(b)(1) requires, in part, that the holders of an operating
      license shall include within the scope of the monitoring program, specified in
      10 CFR 50.65(a)(1), SSCs that are relied upon to remain functional during and following
      design basis events. Contrary to the above, since the combined maintenance rule
      scoping for Units 2 and 3 in 2012, Entergy failed to include within the scope of the
      monitoring program specified in 10 CFR 50.65(a)(1), the safety-related MBFP discharge
      valves. These SSCs are relied upon during and after design basis events to mitigate the
      consequences of a feedwater line break accident inside containment. Entergys
      corrective action included entering this issue into the corrective action program.
      Because the violation was of very low safety significance (Green) and Entergy entered
      this issue into their CAP as CR-IP2-2016-03963, this violation is being treated as an
      NCV, consistent with Section 2.3.2.a of the NRC Enforcement Policy.
      (NCV 05000247/2016002-04, Failure to Scope Safety-Related Main Boiler Feedwater
      Pump Discharge Valves into the Maintenance Rule Program)
4OA5 Other Activities
.1    Groundwater Contamination
  a. Inspection Scope
      On February 5, 2016, Entergy notified the NRC of a significant increase in groundwater
      tritium levels measured at three monitoring wells (MWs) (MW-30, MW-31, and MW-32)
      located near the Unit 2 fuel storage building. These samples were drawn on
      January 26 to 27, 2016, and analyzed and confirmed on February 2 to 4, 2016. The
      highest concentration was detected at MW-32, which increased from 12,000 pCi/l on
      January 11, 2016, to 8,100,000 pCi/l on January 26, 2016, and subsequently up to
      14,800,000 pCi/l on February 4, 2016. This increased tritium concentration event was
      documented by Entergy in CR-IP2-2016-00564 which documents its investigation of this
      event including a root cause evaluation. The inspectors reviewed Entergys root cause
      evaluation for this event during this inspection period as well as recent groundwater
      monitoring results.


J. Taylor, Unit 3 Shift Manager
                                                38
M. Tesoriero, Outage Control Center Manager M. Troy, Nuclear Oversight Manager
b. Findings and Observations
R. Walpole, Regulatory Assurance Manager
  No findings were identified.
A. Zastrow, Assistant Operations Manager
  Update to URI 05000247/2016001-07, January 2016 Groundwater Contamination
  Entergy continues to conduct weekly, biweekly, and monthly groundwater sampling of
  MWs at the initial site of groundwater contamination and at downstream wells towards
  the Hudson River. For the initial three MWs (MW-30, MW-31, and MW-32), the general
  trend in tritium activity has been downward, with periodic increases seen in some weekly
  samples. The downstream MWs located in the Unit 2 switchyard (especially MW-55)
  showed an initial increase in activity up to 117,000 pCi/l, but the activity at that location
  has plateaued at the end of the reporting period.
  Entergy documented its investigation of this event as root cause evaluation for
  CR-IP2-2016-00564. The inspectors reviewed Entergys root cause evaluation for this
  event. Entergy concluded that the source of the groundwater contamination was from
  the reject water of a temporary reverse osmosis unit used to process water from the
  refueling water storage tank at Unit 2 in preparation for RFO 2R22. Although this
  analysis documents a number of issues identified during the operation of the contractor
  reverse osmosis unit, which is believed to be the source of the groundwater
  contamination, one of two leakage paths to groundwater have still not been established.
  The established pathway involves leakage from two cut drain lines located above the
  floor on the 35-foot elevation of the PAB. Further investigation by Entergy following the
  conclusion of the Unit 2 RFO 2R22 must be conducted to verify the second pathway to
  groundwater via the floor of the fuel storage building truck bay.
  Entergys long-term corrective action for reducing tritium levels in the groundwater is the
  same as previously identified for the March 2014 tritium spike (CR-IP2-2015-03806), the
  start-up and operation of recovery well (RW)-1. Following installation of equipment and
  system testing, full operation of the RW system is expected later this year. This system
  will allow for the collection of tritiated groundwater in the vicinity of Unit 2 to be returned
  inside the Unit 2 PAB for processing. The NRC will be conducting an inspection in
  August 2016 to review the testing plan and results of the RW-1 tests. This inspection
  will include a specialist region-based inspector, and a staff hydrogeologist.
  The NRCs continuing assessment of the safety significance of this event focused on
  validating the safety impact of dose to the public from the release of tritium to the site
  groundwater, and ultimately to the Hudson River. The NRC verified that Entergys
  bounding public dose calculations on the groundwater contamination leak was
  sufficiently conservative and a maximum worst case scenario would result in a dose of
  0.000112 millirem per year, which represents a very small fraction of the allowable dose
  (liquid effluent dose objective of 3 millirem per year). This low value is due to
  groundwater at Indian Point not being a source of any drinking water. There are no
  drinking water wells on the Indian Point site, groundwater flow from the site is to the
  Hudson River and not to any near site drinking water wells, and the Hudson River has
  no downstream drinking water intakes as it is brackish water. Pathways to the public are
  therefore limited to the consumption of fish and river invertebrates. The inspection
  determined that there is no safety impact to the public as a result of this groundwater
  contamination event. (URI 05000247/2016001-07, January 2016 Groundwater
  Contamination)


    
                                              39
A-2  LIST OF ITEMS OPENED, CLOSED, DISCUSSED, AND UPDATED
.2   Institute of Nuclear Power Operations (INPO) Report Review
  Opened 
  a. Inspection Scope
05000247/2016002-01 URI  CVCS Goal Monitoring Under the Maintenance
      The inspectors also reviewed the final report for the INPO equipment reliability scram
       Rule (Section 1R12)
      review visit that was conducted to review the scrams that occurred over the past two
      years, conducted in June 2016. The inspectors reviewed the report to ensure that any
      issues identified were consistent with NRC perspectives of Entergy performance and to
      determine if INPO identified any significant safety issues that required further NRC
      follow-up.
  b. Findings
      No findings were identified.
4OA6 Meetings, Including Exit
      On August 4, 2016, the inspectors presented the inspection results to Mr. Larry Coyle,
      Site Vice President, and other members of Entergy. Based on additional information
      provided, the inspectors conducted an updated exit meeting on August 30, 2016 with
      John Kirkpatrick, Plant Operations General Manager and other members of Entergy.
      The inspectors verified that no proprietary information was retained by the inspectors or
       documented in this report.
ATTACHMENT: SUPPLEMENTARY INFORMATION


                                              A-1
Opened/Closed
                                SUPPLEMENTARY INFORMATION
05000286/2016002-02 NCV  Failure to Follow Operability Determination
                                  KEY POINTS OF CONTACT
Procedure for Unit 3 Baffle-Former Bolts
Entergy Personnel
(Section 1R15)
A. Vitale, Site Vice President
J. Kirkpatrick, Plant Operations General Manager
05000247/2016002-03 NCV  Failure to Maintain Flow Channeling Gates Closed in Accordance with the Containment Procedure (Section 1R20)
R. Alexander, Unit 2 Shift Manager
R. Andersen, Maintenance Instrumentation and Controls Superintendent
05000247/2016002-04 NCV  Failure to Scope Safety-Related Main Boiler
N. Azevedo, Engineering Supervisor
      Feedwater Pump Discharge Valves into the
J. Baker, Shift Manager
Maintenance Rule Program (Section 4OA3)
S. Bianco, Operations Fire Marshal
K. Brooks, Assistant Operations Manager
Closed 
R. Burroni, Engineering Director
05000247/2015-003-00 LER  Manual Reactor Trip due to Indications of Multiple
T. Chan, Engineering Supervisor
      Dropped Control Rods Caused by Loss of Control      Rod Power Due to a Power Supply Failure (Section 4OA3)
C. Chapin, Training Superintendent
D. Dewey, Assistant Operations Manager
05000247/2016-003-00 LER  Technical Specification Prohibited Condition Due to an Inoperable 21 Main Boiler Feedwater
J. Dignam, Unit 3 Control Room Supervisor
Pump Discharge Valve for Greater Than the TS
R. Dolansky, Inservice Inspection Program Manager
Allowed Outage Time (Section 4OA3)
W. Durr, Outage Control Center Manager
R. Drake, Engineering Supervisor
Discussed
K. Elliott, Fire Protection Engineer
J. Ferrick, Regulatory and Performance Improvement Director
05000247/2016001-01 URI Baffle-Former Bolts with Identified Anomalies  (Section 1R08)
L. Frink, Radiation Protection Supervisor
D. Gagnon, Security Manager
05000247/2016001-06 URI Emergency Diesel Generator Automatic Voltage
L. Glander, Emergency Preparedness Manager
Regulator Failure (Section 1R15)
D. Gray, Radiological Environmental Manager
05000247/2016001-07 URI  January 2016 Groundwater Contamination        Section (Section 4OA5)
J. Johnson, Unit 2 Control Room Supervisor
 
M. Johnson, Unit 3 Shift Manager
A-3  LIST OF DOCUMENTS REVIEWED
M. Khadabux, Instrumentation and Controls Supervisor
 
F. Kich, Performance Improvement Manager
Common Documents Used Indian Point Unit 2 and Unit 3, UFSARs
M. Lewis, Unit 3 Assistant Operations Manager
Indian Point Unit 2 and Unit 3, Individual Plant Examinations
N. Lizzo, Training Manager
Indian Point Unit 2 and Unit 3, Individual Plant Examination of External Events
S. McAllister, Baffle Bolt Replacement Project Manager
Indian Point Unit 2 and Unit 3, TSs and Bases
M. McCarthy, Unit 3 Control Room Supervisor
Indian Point Unit 2 and Unit 3, Technical Requirements Manuals
B. McCarthy, Operations Manager
Indian Point Unit 2 and Unit 3, Control Room Narrative Logs Indian Point Unit 2 and Unit 3, Plans of the Day
F. Mitchell, Radiation Protection Manager
Section 1R04:  Equipment Alignment
E. Mullek, Maintenance Manager
  Procedures 2-COL-4.2.1, Residual Heat Removal System, Revision 30
S. Stevens, Radiation Protection Operations Superintendent
2-COL-4.3.1, Spent Fuel Pit Cooling, Revision 10
B. Sullivan, Training Superintendent
2-COL-24.1.1, Service Water System, Revision 50
J. Taylor, Unit 3 Shift Manager
3-COL-EL-005, Diesel Generators, Revision 37
M. Tesoriero, Outage Control Center Manager
OAP-019, Component Verification and System Status Control, Revision 7 OAP-044, Plant Labeling Program, Revision 3
M. Troy, Nuclear Oversight Manager
R. Walpole, Regulatory Assurance Manager
Condition Reports (CR-IP2)
A. Zastrow, Assistant Operations Manager
2016-01311 2016-01505 2016-01761 2016-02330 2016-02428 2016-02470
                                                                    Attachment


                                    A-2
Condition Reports (CR-IP3)  
          LIST OF ITEMS OPENED, CLOSED, DISCUSSED, AND UPDATED
2016-01382 2016-01810
Opened
05000247/2016002-01    URI        CVCS Goal Monitoring Under the Maintenance
                                  Rule (Section 1R12)
Opened/Closed
05000286/2016002-02    NCV        Failure to Follow Operability Determination
                                  Procedure for Unit 3 Baffle-Former Bolts
                                  (Section 1R15)
05000247/2016002-03    NCV        Failure to Maintain Flow Channeling Gates Closed
                                  in Accordance with the Containment Procedure
                                  (Section 1R20)
05000247/2016002-04    NCV        Failure to Scope Safety-Related Main Boiler
                                  Feedwater Pump Discharge Valves into the
                                  Maintenance Rule Program (Section 4OA3)
Closed
05000247/2015-003-00    LER        Manual Reactor Trip due to Indications of Multiple
                                  Dropped Control Rods Caused by Loss of Control
                                  Rod Power Due to a Power Supply Failure
                                  (Section 4OA3)
05000247/2016-003-00    LER        Technical Specification Prohibited Condition
                                  Due to an Inoperable 21 Main Boiler Feedwater
                                  Pump Discharge Valve for Greater Than the TS
                                  Allowed Outage Time (Section 4OA3)
Discussed
05000247/2016001-01    URI        Baffle-Former Bolts with Identified Anomalies
                                  (Section 1R08)
05000247/2016001-06    URI        Emergency Diesel Generator Automatic Voltage
                                  Regulator Failure (Section 1R15)
05000247/2016001-07    URI        January 2016 Groundwater Contamination
                                  Section (Section 4OA5)


                                                A-3
Drawings 209762, Flow Diagram Service Water System Nuclear Steam Supply Plant, Revision 75  
                              LIST OF DOCUMENTS REVIEWED
227781, Flow Diagram Auxiliary Coolant System, Revision 22 9321-2720, Auxiliary Coolant System, Sheet 2, Revision 22  
Common Documents Used
Indian Point Unit 2 and Unit 3, UFSARs
Miscellaneous IP3-DBD-308, CCW System, Revision 3  
Indian Point Unit 2 and Unit 3, Individual Plant Examinations
Indian Point Unit 2 and Unit 3, Individual Plant Examination of External Events
Indian Point Unit 2 and Unit 3, TSs and Bases
Indian Point Unit 2 and Unit 3, Technical Requirements Manuals
Indian Point Unit 2 and Unit 3, Control Room Narrative Logs
Indian Point Unit 2 and Unit 3, Plans of the Day
Section 1R04: Equipment Alignment
Procedures
2-COL-4.2.1, Residual Heat Removal System, Revision 30
2-COL-4.3.1, Spent Fuel Pit Cooling, Revision 10
2-COL-24.1.1, Service Water System, Revision 50
3-COL-EL-005, Diesel Generators, Revision 37
OAP-019, Component Verification and System Status Control, Revision 7
OAP-044, Plant Labeling Program, Revision 3
Condition Reports (CR-IP2)
2016-01311 2016-01505 2016-01761              2016-02330    2016-02428    2016-02470
Condition Reports (CR-IP3)
2016-01382 2016-01810
Drawings
209762, Flow Diagram Service Water System Nuclear Steam Supply Plant, Revision 75
227781, Flow Diagram Auxiliary Coolant System, Revision 22
9321-2720, Auxiliary Coolant System, Sheet 2, Revision 22
Miscellaneous
IP3-DBD-308, CCW System, Revision 3
Section 1R05: Fire Protection
Procedures
EN-MA-133, Control of Scaffolding, Revision 12
Condition Reports (CR-IP2)
2016-04148
Condition Reports (CR-IP3)
2016-01272
Miscellaneous
PFP-203, Containment Building, 95-Foot Elevation (Fire Zone 86A), Revision 15
PFP-204, General Floor Plan, PAB, 15-Foot Elevation, Revision 0
PFP-209, Component Cooling Pump Room, PAB, 68-Foot Elevation, Revision 0
PFP-211, General Floor Plan, PAB, 80-Foot Elevation, Revision 14
PFP-351, 480V Switchgear Room, Revision 15


Section 1R05: Fire Protection
                                                A-4
  Procedures EN-MA-133, Control of Scaffolding, Revision 12
Section 1R07: Heat Sink Performance
Procedures
0-HTX-405-EDG, EDG Lube Oil and Jacket Water Heat Exchanger Maintenance, Revision 4
Condition Reports (CR-IP3)
2010-02900 2011-03594          2011-03596    2011-03961    2012-02071      2012-03912
2013-02338 2013-02695          2013-03009    2014-00957    2014-01239      2014-03158
2014-03175 2015-00031          2015-00599    2015-02848    2015-05209      2015-05526
2016-00886 2016-00895          2016-00899
Maintenance Orders/Work Orders
WO 52489888            WO 52626563
Miscellaneous
SEP-SW-IPC-001, Indian Point Energy Center NRC Generic Letter 89-13 Service Water
        Program, Revision 0
Section 1R08: Inservice Inspection Activities
Procedures
GBRA-104-659, Collection of Protocols for Baffle Bolt Replacement, Revision C
GBRA-175-115, Field Service Procedure for Baffle Bolt Replacement, Revision 3
WDI-STD-088, Underwater Remote Visual Examination of Reactor Vessel Internals,
    Revision 13
WDI-STD-1073, Ultrasonic Test Procedure for the Inspection of Internal Hex Head
    Baffle-Former Bolts with Welded Lock Bars, Revision 4
Condition Reports (CR-IP2)
2016-02081
Maintenance Orders/Work Orders
442412-13
Miscellaneous
Indian Point Unit 2 Baffle Bolt Ultrasonic Examination Expanded Analysis Report, dated
    April 28, 2016
IP2 Reactor Vessel Visual Examination Report, dated May 2006
Loose Parts Inventory Log for Baffle Bolt Replacements, dated May 24, 2016
MRP-227-A, Materials Reliability Program: Pressurized Water Reactor Internals Inspection and
    Evaluation Guidelines (ML120170453)
MRP-228, Materials Reliability Program: Inspection Standard for PWR Internals - 2012 Update,
    Revision 1
SEP-ISI-IP2-001, IP2 Fourth Ten-Year Interval Inservice Inspection (ISI)/Containment Inservice
    Inspection (CISI) Program Plan, Revision 2
WDI-PJF-1315504-EPP-001, Indian Point Nuclear Power Plant MRP-227-A Reactor Vessel
    Internals Examination Program Plan, Revision 0
WDI-PJF-1315505-FSR-001, Indian Point Unit 2 2R22 MRP-227-A Baffle-Former Bolt
    Ultrasonic Inspections Field Service Report, dated March 29, 2016
WDI-TJ-1100, Technical Justification for the Ultrasonic Inspection of Baffle-Former Bolts for
    Indian Point Units 2 and 3, Revision 1


                                                A-5
Condition Reports (CR-IP2)
Section 1R11: Licensed Operator Requalification Program
2016-04148
Procedures
 
2-AOP-480V-1, Loss of Normal Power to Any 480V Vital Bus, Revision 8
2-AOP-RCP-1, Reactor Coolant Pump Malfunction, Revision 14
Condition Reports (CR-IP3)
2-AOP-TURB-1, Main Turbine Trip without a Reactor Trip, Revision 5
2016-01272
2-E-0, Reactor Trip or Safety Injection, Revision 7
 
2-FR-H.1, Response to Loss of Secondary Heat Sink, Revision 11
2-POP-1.2, Reactor Startup, Revision 59
Miscellaneous PFP-203, Containment Building, 95-Foot Elevation (Fire Zone 86A), Revision 15
2-SOP-26.4, Turbine Generator Startup, Synchronizing, Voltage Control and Shutdown,
PFP-204, General Floor Plan, PAB, 15-Foot Elevation, Revision 0
      Revision 62
PFP-209, Component Cooling Pump Room, PAB, 68-Foot Elevation, Revision 0
3-AOP-480V-1, Loss of Normal Power to Any Safeguards Bus, Revision 7
PFP-211, General Floor Plan, PAB, 80-Foot Elevation, Revision 14
3-AOP-CVCS-1, Chemical and Volume Control System Malfunction, Revision 8
PFP-351, 480V Switchgear Room, Revision 15
3-AOP-FW-1, Loss of Feedwater, Revision 8
 
3-AOP-INST-1, Instrument/Controller Failures, Revision 11
A-4  Section 1R07:  Heat Sink Performance
3-E-0, Reactor Trip or Safety Injection, Revision 6
Procedures 0-HTX-405-EDG, EDG Lube Oil and Jacket Water Heat Exchanger Maintenance, Revision 4
3-E-1, Loss of Reactor or Secondary Coolant, Revision 4
 
3-FR-C.2, Response to Degraded Core Cooling, Revision 3
Condition Reports (CR-IP2)
Condition Reports (CR-IP3)
2016-03946 2016-04162 2016-04164             2016-04165 2016-04169   2016-04178
2010-02900 2011-03594 2011-03596 2011-03961 2012-02071 2012-03912
Condition Reports (CR-IP3)
 
2016-01087 2016-01092 2016-01098             2016-01336
2013-02338 2013-02695 2013-03009 2014-00957 2014-01239 2014-03158
Miscellaneous
 
13SX-LOR-SES026, Licensed Operator Requalification Program Scenario
2014-03175 2015-00031 2015-00599 2015-02848 2015-05209 2015-05526
Emergency Action Level Table, Revision 15.2
2016-00886 2016-00895 2016-00899
Maintenance Orders/Work Orders WO 52489888  WO 52626563
 
Miscellaneous SEP-SW-IPC-001, Indian Point Energy Center NRC Generic Letter 89-13 Service Water
Program, Revision 0
Section 1R08:  Inservice Inspection Activities
Procedures GBRA-104-659, Collection of Protocols for Baffle Bolt Replacement, Revision C
GBRA-175-115, Field Service Procedure for Baffle Bolt Replacement, Revision 3
WDI-STD-088, Underwater Remote Visual Examination of Reactor Vessel Internals, Revision 13 WDI-STD-1073, Ultrasonic Test Procedure for the Inspection of Internal Hex Head Baffle-Former Bolts with Welded Lock Bars, Revision 4
Condition Reports (CR-IP2)
2016-02081
Maintenance Orders/Work Orders
442412-13
 
Miscellaneous Indian Point Unit 2 Baffle Bolt Ultrasonic Examination Expanded Analysis Report, dated April 28, 2016 IP2 Reactor Vessel Visual Examination Report, dated May 2006
Loose Parts Inventory Log for Baffle Bolt Replacements, dated May 24, 2016
MRP-227-A, Materials Reliability Program:  Pressurized Water Reactor Internals Inspection and Evaluation Guidelines (ML120170453) MRP-228, Materials Reliability Program:  Inspection Standard for PWR Internals - 2012 Update, Revision 1 SEP-ISI-IP2-001, IP2 Fourth Ten-Year Interval Inservice Inspection (ISI)/Containment Inservice Inspection (CISI) Program Plan, Revision 2 WDI-PJF-1315504-EPP-001, Indian Point Nuclear Power Plant MRP-227-A Reactor Vessel Internals Examination Program Plan, Revision 0 WDI-PJF-1315505-FSR-001, Indian Point Unit 2 2R22 MRP-227-A Baffle-Former Bolt Ultrasonic Inspections Field Service Report, dated March 29, 2016 WDI-TJ-1100, Technical Justification for the Ultrasonic Inspection of Baffle-Former Bolts for Indian Point Units 2 and 3, Revision 1
 
A-5  Section 1R11: Licensed Operator Requalification Program  
Procedures 2-AOP-480V-1, Loss of Normal Power to Any 480V Vital Bus, Revision 8  
 
2-AOP-RCP-1, Reactor Coolant Pump Malfunction, Revision 14
2-AOP-TURB-1, Main Turbine Trip without a Reactor Trip, Revision 5  
 
2-E-0, Reactor Trip or Safety Injection, Revision 7  
2-FR-H.1, Response to Loss of Secondary Heat Sink, Revision 11  
2-POP-1.2, Reactor Startup, Revision 59 2-SOP-26.4, Turbine Generator Startup, Synchronizing, Voltage Control and Shutdown, Revision 62 3-AOP-480V-1, Loss of Normal Power to Any Safeguards Bus, Revision 7  
3-AOP-CVCS-1, Chemical and Volume Control System Malfunction, Revision 8  
3-AOP-FW-1, Loss of Feedwater, Revision 8 3-AOP-INST-1, Instrument/Controller Failures, Revision 11  
3-E-0, Reactor Trip or Safety Injection, Revision 6  
3-E-1, Loss of Reactor or Secondary Coolant, Revision 4  
3-FR-C.2, Response to Degraded Core Cooling, Revision 3  
 
Condition Reports (CR-IP2)  
2016-03946 2016-04162 2016-04164 2016-04165 2016-04169 2016-04178  
Condition Reports (CR-IP3)  
2016-01087 2016-01092 2016-01098 2016-01336  
 
Miscellaneous 13SX-LOR-SES026, Licensed Operator Requalification Program Scenario Emergency Action Level Table, Revision 15.2  
LRQ-SES-04, IPEC Simulator Evaluated Scenario, Revision 6
LRQ-SES-04, IPEC Simulator Evaluated Scenario, Revision 6
  Section 1R12: Maintenance Effectiveness
Section 1R12: Maintenance Effectiveness
  Procedures CEP-NDE-0640, Non-Section XI Liquid Penetrant Examination, Revision 9  
Procedures
CEP-WP-WIIR-1, Attachment 5.1, Inprocess Inspections for Installation and Replacement Welds Located Inside the ASME Section XI Boundary, Revision 3 EN-DC-206, Maintenance Rule (a)(1) Process, Revision 3  
CEP-NDE-0640, Non-Section XI Liquid Penetrant Examination, Revision 9
CEP-WP-WIIR-1, Attachment 5.1, Inprocess Inspections for Installation and Replacement
Condition Reports (CR-IP2) 2010-00864 2013-03130 2014-00162 2014-00185 2014-01144 2014-02184
  Welds Located Inside the ASME Section XI Boundary, Revision 3
 
EN-DC-206, Maintenance Rule (a)(1) Process, Revision 3
2015-00278 2016-01260 2016-01430 2016-01500  
Condition Reports (CR-IP2)
Condition Reports (CR-IP3)  
2010-00864 2013-03130 2014-00162             2014-00185 2014-01144   2014-02184
2012-03836 2013-04758 2015-01396 2015-03404 2015-03653 2015-04053  
2015-00278 2016-01260 2016-01430             2016-01500
 
Condition Reports (CR-IP3)
2015-04162 2015-04184 2015-04539 2015-05316 2015-05384 2015-05729  
2012-03836 2013-04758 2015-01396             2015-03404 2015-03653   2015-04053
 
2015-04162 2015-04184 2015-04539             2015-05316 2015-05384   2015-05729
 
A-6  2016-00098 2016-00653 2016-00723 2016-01189 2016-01227 2016-01274
2016-01313 2016-01531 2016-01536 2016-01543 2016-02432 
 
Maintenance Orders/Work Orders WO 00397793  WO 00408019  WO 00414886  WO 00416091 WO 00421841  WO 00429532  WO 00429532  WO 00431497
WO 00446165  WO 00447042  WO 00447966  WO 52602429
 
WO 52621178
 
Miscellaneous EC 65389, 21 CCW HX Leak Repair: Service Water Inlet Nozzle - Elbow Weld Configuration
Change IPEC Maintenance Rule Basis Document - Chemical and Volume Control System, Revision 0
PQR 913, 134 F42 MN-GTAW ASME IX Welding Procedure Qualification Record, Revision 0 System Health Report, Unit 3, EDG, Q1-2016
Weld Map Number 447966-20-01, Revision 0
WPS 134 F42, MN-GTAW, ASME Section IX Welding Procedure Specification, Revision 0
 
Section 1R13:  Maintenance Risk Assessments and Emergent Work Control
  Procedures
EN-OP-119, Protected Equipment, Revision 8
 
IP-SMM-OU-104, Attachment 9.1, Shiftly Ou
tage Shutdown Safety Assessments, Revision 15
IP-SMM-OU-104, Attachment 9.2, Shiftly Ou
tage Shutdown Safety Assessment Guidelines, Revision 15
Condition Reports (CR-IP2)
2016-04141
 
Condition Reports (CR-IP3)
2016-01545
 
Miscellaneous EOOS Risk Assessment Software Tool
Section 1R15:  Operability Determinations and Functionality Assessments
  Procedures 2-PC-R3-1, Pressurizer Level Transmitters, Revision 10
3-ARP-010, Metal Impact Monitoring System, Page 10, Revision 32
3-SOP-RCS-016, Operation of the Metal Impact Monitoring System, Revision 8 EN-OP-104, Operability Determination Process, Revision 10 
Condition Reports (CR-IP2) 2016-2221 2016-2356 2016-2961 2016-3345 2016-3418 2016-3660 
 
2016-3636 2016-3784 2016-3806 2016-3818 2016-4085
 
Condition Reports (CR-IP3)
2014-01670 2015-03468
 
A-7  Maintenance Orders/Work Orders WO 00327574  WO 00425980  WO 52571030
Miscellaneous
EN-LI-100, Attachment 9.1, Change Channel Check Comparison Criteria/2-PT-M100, 2-PT-D001, Revision 0
Section 1R18:  Plant Modifications
Drawings 10073E87-001, Indian Point Unit 2 Baffle Bolt Replacement - Core Barrel and Baffle Assembly
Elevation, Revision 0 10111D06, Indian Point Unit 2 Baffle Bolt Replacement - Replacement Baffle Bolt .625
and .750, Revision 0
Miscellaneous EC 64308, IP2 Reactor Vessel Equivalent Replacement Baffle-to-Former Bolt, Revision 0
Process Applicability Determination Form for EC 64308, dated April 21, 2016
WCAP-18136-P, Replacement Type 316 Cold-Worked Baffle-Former Bolt Qualification for Indian Point Unit 2, Revision 0
Section 1R19:  Post-Maintenance Testing
  Procedures 3-PT-M079B, 32 EDG Functional Test, Revision 52 2-PC-Q109-4, Recalibration of NIS and OT/OP Delta-T Parameters - Channel IV, Revision 44
Condition Reports (CR-IP2)
2016-03961 2016-04266
 
Condition Reports (CR-IP3)
2016-01189 2016-01199 2016-01218
Maintenance Orders/Work Orders WO 00414886  WO 00420649  WO 00446094  WO 00447966
WO 52545181  WO 52626563  WO 52626564  WO 52630619 WO 52630620  WO 52658943  WO 00236158  WO 00277374
WO 52571030
 
Drawings 5651D72, Logic Diagrams Steam Generator Trip Signals, Revision 7
Miscellaneous EC 64545, Emergency Temporary Modification to Disconnect 32 EDG Generator Space Heater Adjacent to End Plate on Outboard End of Generator FIX00091, Pressurizer Level Uncertainty - Indication, Trip Setpoints, and Annunciation 
Setpoints, Revision 1 E-mail from J. Michetti to G. Newman, dated July 19, 2016, Subject:  Westinghouse Report
on E9   
A-8  Section 1R20:  Refueling and Other Outage Activities
Procedures 2-POP-1.1, Plant Heatup from Cold Shutdown, Revision 90
2-POP-1.2, Reactor Startup, Revision 59
2-POP-1.3, Plant Startup from Zero to 45 Percent Power, Revision 89
2-POP-3.1, Plant Shutdown from 45 Percent Power, Revision 58
2-POP-3.3, Plant Cooldown, Hot to Cold Shutdown, Revision 81
2-POP-3.4, Secondary Plant Shutdown, Revision 10 2-POP-4.1, Operation at Cold Shutdown, Revision 5 2-POP-4.2, Operation Below 20 Percent Pressurizer Level with Fuel in the Reactor, Revision 8
2-POP-4.3, Operation without Fuel in the Reactor, Revision 1
 
Condition Reports (CR-IP2-)
2016-04118 2016-04119 2016-04123 2016-03124 2016-04126 2016-04129
2016-04130 2016-04131 2016-04132 2016-04139 2016-04141* 2016-04142*
2016-04144 2016-04145 2016-04146 2016-04148* 2016-04151 2016-04152
 
2016-04155 2016-04161 2016-04162 2016-04165 2016-04169
 
*NRC identified
Maintenance Orders/Work Orders
52681465
Miscellaneous 2R22 Performance Indicator Curves Daily from March 7 to June 14, 2016
Outage Schedules and Plans of the Day from March 7 to June 14, 2016
Westinghouse LTR-PL-16-16, Operability Assessment for Primary Side Loose Parts at Indian
Point Unit 2, Revision 0, dated March 27, 2016
Section 1R22:  Surveillance Testing
  Procedures 0-SOP-LEAKRATE-001, RCS Leakrate Surveillance Evaluation and Leak Identification, Revision 6 2-PT-D001, Control Room Operations Surveillance Requirements, Revision 16 2-PT-M029B, 22 Safety Injection Pump, Revision 20 2-PT-Q013, Inservice Valve Tests, Revision 51
2-PT-Q013-DS040, Valve 887B Inservice Test Data Sheet, Revision 22
3-PT-M079B, 32 EDG Functional Test, Revision 52
 
Condition Reports (CR-IP2)
2016-03360 2016-03363
Condition Reports (CR-IP3)
2016-01716 2016-01752
 
Maintenance Orders/Work Orders WO 00443040  WO 00446385  WO 00446867  WO 52681652-01
WO 52681646-01
 
 
A-9  Miscellaneous EC 64855, EC Reply to Provide Input Regarding MPR Maintenance Bulletin MB-2007-01 for Auto Voltage Regulator Solder Joints MB-2007-01, Potential for Solder Joint Cracks on Basler SBSR Auto Voltage Regulator Cards and Technical Manual Addendum TM-2007-01, November 5, 2007 Unit 3 RCS Routine Activity Sample, 28-June-16-10006
Section 1EP6:  Drill Evaluation
Procedures IP-EP-120, Emergency Classification, Revision 10 IP-EP-410, Protective Action Recommendations, Revision 11
 
Section 2RS7:  Radiological Environmental Monitoring Program
Procedures
0-CY-1920, REMP Land Use Census, Revision 1
0-CY-1980, Preparation, Placement and Collection of Site Environmental Thermoluminescent
Dosimeters, Revision 2
Condition Reports (CR-IP2)
2014-05319 2015-00948 2015-01300 2015-02687 2015-02800 2015-02987
 
2015-03271 2015-03396 2016-02313
 
Condition Reports (CR-IP3)
2016-00514
 
Miscellaneous 2014 Annual Radiological Environmental Operating Report, Indian Point Nos. 1, 2, and 3
2015 Annual Radiological Environmental Operating Report, Indian Point Nos. 1, 2, and 3 Environmental Dosimetry Company, Annual Quality Assurance Status Report, January to December 2015 Indian Point Energy Center ODCM, Revision 4
June 2015 to May 2016 Meteorological Data Recovery
Met One Instruments, Inc. Certificates of Calibration for Temperature, Wind Direction, and Wind
Speed Teledyne Brown Engineering Environmental Serv
ices Annual 2015 Quality Assurance Report
Exelon PowerLabs Certificates of Calibration for Gas Meters
3471875 3482909 3471871 3471867 3482920 3471873


3482910 3482916 3471877 3482914 3482918 3482921
                                            A-6
3471881 3471879 3471872 3471869 3471880 3482908
2016-00098    2016-00653    2016-00723    2016-01189  2016-01227  2016-01274
2016-01313    2016-01531    2016-01536    2016-01543  2016-02432
Quality Assurance
Maintenance Orders/Work Orders
Quality Assurance Audit Report QA-2-6-2015-IP-1, Chemistry, Effluents, and Environmental Monitoring Snapshot Self-Assessment, LO-IP3LO-2015-00126, Chemistry-REMP
WO 00397793          WO 00408019          WO 00414886        WO 00416091
WO 00421841          WO 00429532          WO 00429532        WO 00431497
Section 4OA2: Problem Identification and Resolution
WO 00446165          WO 00447042          WO 00447966        WO 52602429
  Procedures EN-DC-204, Maintenance Rule Scope and Basis, Revision 3
WO 52621178
EN-DC-204, Maintenance Rule Scope and Basis, Revision 3 EN-DC-207, Maintenance Rule Periodic Assessment, Revision
Miscellaneous
A-10  EN-LI-102, Corrective Action Program, Revision 26 EN-LI-104, Self-Assessment and Benchmark Process, Revision 11
EC 65389, 21 CCW HX Leak Repair: Service Water Inlet Nozzle - Elbow Weld Configuration
EN-LI-110-01, Equipment Failure Evaluation, Revision 0
      Change
EN-LI-119, Apparent Cause Evaluation Process, Revision 11 EN-OP-104, Operability Determination Process, Revision 10  
IPEC Maintenance Rule Basis Document - Chemical and Volume Control System, Revision 0
PQR 913, 134 F42 MN-GTAW ASME IX Welding Procedure Qualification Record, Revision 0
System Health Report, Unit 3, EDG, Q1-2016
Weld Map Number 447966-20-01, Revision 0
WPS 134 F42, MN-GTAW, ASME Section IX Welding Procedure Specification, Revision 0
Section 1R13: Maintenance Risk Assessments and Emergent Work Control
Procedures
EN-OP-119, Protected Equipment, Revision 8
IP-SMM-OU-104, Attachment 9.1, Shiftly Outage Shutdown Safety Assessments, Revision 15
IP-SMM-OU-104, Attachment 9.2, Shiftly Outage Shutdown Safety Assessment Guidelines,
      Revision 15
Condition Reports (CR-IP2)
2016-04141
Condition Reports (CR-IP3)
2016-01545
Miscellaneous
EOOS Risk Assessment Software Tool
Section 1R15: Operability Determinations and Functionality Assessments
Procedures
2-PC-R3-1, Pressurizer Level Transmitters, Revision 10
3-ARP-010, Metal Impact Monitoring System, Page 10, Revision 32
3-SOP-RCS-016, Operation of the Metal Impact Monitoring System, Revision 8
EN-OP-104, Operability Determination Process, Revision 10
Condition Reports (CR-IP2)
2016-2221    2016-2356    2016-2961      2016-3345    2016-3418    2016-3660
2016-3636    2016-3784    2016-3806      2016-3818    2016-4085
Condition Reports (CR-IP3)
2014-01670 2015-03468


                                              A-7
Condition Reports (CR-IP2)  
Maintenance Orders/Work Orders
2010-07013 2015-04574 2015-05458 2015-05460 2015-05461 2015-05464
WO 00327574            WO 00425980          WO 52571030
Miscellaneous
EN-LI-100, Attachment 9.1, Change Channel Check Comparison Criteria/2-PT-M100,
  2-PT-D001, Revision 0
Section 1R18: Plant Modifications
Drawings
10073E87-001, Indian Point Unit 2 Baffle Bolt Replacement - Core Barrel and Baffle Assembly
    Elevation, Revision 0
10111D06, Indian Point Unit 2 Baffle Bolt Replacement - Replacement Baffle Bolt .625
    and .750, Revision 0
Miscellaneous
EC 64308, IP2 Reactor Vessel Equivalent Replacement Baffle-to-Former Bolt, Revision 0
Process Applicability Determination Form for EC 64308, dated April 21, 2016
WCAP-18136-P, Replacement Type 316 Cold-Worked Baffle-Former Bolt Qualification for
    Indian Point Unit 2, Revision 0
Section 1R19: Post-Maintenance Testing
Procedures
3-PT-M079B, 32 EDG Functional Test, Revision 52
2-PC-Q109-4, Recalibration of NIS and OT/OP Delta-T Parameters - Channel IV, Revision 44
Condition Reports (CR-IP2)
2016-03961 2016-04266
Condition Reports (CR-IP3)
2016-01189 2016-01199 2016-01218
Maintenance Orders/Work Orders
WO 00414886            WO 00420649          WO 00446094            WO 00447966
WO 52545181            WO 52626563          WO 52626564            WO 52630619
WO 52630620            WO 52658943          WO 00236158            WO 00277374
WO 52571030
Drawings
5651D72, Logic Diagrams Steam Generator Trip Signals, Revision 7
Miscellaneous
EC 64545, Emergency Temporary Modification to Disconnect 32 EDG Generator Space Heater
        Adjacent to End Plate on Outboard End of Generator
FIX00091, Pressurizer Level Uncertainty - Indication, Trip Setpoints, and Annunciation
        Setpoints, Revision 1
E-mail from J. Michetti to G. Newman, dated July 19, 2016, Subject: Westinghouse Report
        on E9


2015-05466 2015-05467 2016-01374 2016-02348
                                              A-8
Condition Reports (CR-IP3) 2015-3628 2016-01035 2016-01961
Section 1R20: Refueling and Other Outage Activities
Procedures
2-POP-1.1, Plant Heatup from Cold Shutdown, Revision 90
2-POP-1.2, Reactor Startup, Revision 59
2-POP-1.3, Plant Startup from Zero to 45 Percent Power, Revision 89
2-POP-3.1, Plant Shutdown from 45 Percent Power, Revision 58
2-POP-3.3, Plant Cooldown, Hot to Cold Shutdown, Revision 81
2-POP-3.4, Secondary Plant Shutdown, Revision 10
2-POP-4.1, Operation at Cold Shutdown, Revision 5
2-POP-4.2, Operation Below 20 Percent Pressurizer Level with Fuel in the Reactor, Revision 8
2-POP-4.3, Operation without Fuel in the Reactor, Revision 1
Condition Reports (CR-IP2-)
2016-04118 2016-04119        2016-04123    2016-03124    2016-04126 2016-04129
2016-04130 2016-04131        2016-04132    2016-04139    2016-04141* 2016-04142*
2016-04144 2016-04145        2016-04146    2016-04148*  2016-04151 2016-04152
2016-04155 2016-04161        2016-04162    2016-04165    2016-04169
*NRC identified
Maintenance Orders/Work Orders
52681465
Miscellaneous
2R22 Performance Indicator Curves Daily from March 7 to June 14, 2016
Outage Schedules and Plans of the Day from March 7 to June 14, 2016
Westinghouse LTR-PL-16-16, Operability Assessment for Primary Side Loose Parts at Indian
      Point Unit 2, Revision 0, dated March 27, 2016
Section 1R22: Surveillance Testing
Procedures
0-SOP-LEAKRATE-001, RCS Leakrate Surveillance Evaluation and Leak Identification,
      Revision 6
2-PT-D001, Control Room Operations Surveillance Requirements, Revision 16
2-PT-M029B, 22 Safety Injection Pump, Revision 20
2-PT-Q013, Inservice Valve Tests, Revision 51
2-PT-Q013-DS040, Valve 887B Inservice Test Data Sheet, Revision 22
3-PT-M079B, 32 EDG Functional Test, Revision 52
Condition Reports (CR-IP2)
2016-03360 2016-03363
Condition Reports (CR-IP3)
2016-01716 2016-01752
Maintenance Orders/Work Orders
WO 00443040          WO 00446385          WO 00446867        WO 52681652-01
WO 52681646-01


                                              A-9
Maintenance Orders/Work Orders
Miscellaneous
WO 00442412
EC 64855, EC Reply to Provide Input Regarding MPR Maintenance Bulletin MB-2007-01 for
        Auto Voltage Regulator Solder Joints
MB-2007-01, Potential for Solder Joint Cracks on Basler SBSR Auto Voltage Regulator Cards
        and Technical Manual Addendum TM-2007-01, November 5, 2007
Unit 3 RCS Routine Activity Sample, 28-June-16-10006
Section 1EP6: Drill Evaluation
Procedures
IP-EP-120, Emergency Classification, Revision 10
IP-EP-410, Protective Action Recommendations, Revision 11
Section 2RS7: Radiological Environmental Monitoring Program
Procedures
0-CY-1920, REMP Land Use Census, Revision 1
0-CY-1980, Preparation, Placement and Collection of Site Environmental Thermoluminescent
        Dosimeters, Revision 2
Condition Reports (CR-IP2)
2014-05319 2015-00948 2015-01300            2015-02687    2015-02800    2015-02987
2015-03271 2015-03396 2016-02313
Condition Reports (CR-IP3)
2016-00514
Miscellaneous
2014 Annual Radiological Environmental Operating Report, Indian Point Nos. 1, 2, and 3
2015 Annual Radiological Environmental Operating Report, Indian Point Nos. 1, 2, and 3
Environmental Dosimetry Company, Annual Quality Assurance Status Report,
        January to December 2015
Indian Point Energy Center ODCM, Revision 4
June 2015 to May 2016 Meteorological Data Recovery
Met One Instruments, Inc. Certificates of Calibration for Temperature, Wind Direction, and Wind
        Speed
Teledyne Brown Engineering Environmental Services Annual 2015 Quality Assurance Report
Exelon PowerLabs Certificates of Calibration for Gas Meters
3471875        3482909      3471871        3471867        3482920      3471873
3482910        3482916      3471877        3482914        3482918      3482921
3471881        3471879      3471872        3471869        3471880      3482908
Quality Assurance
Quality Assurance Audit Report QA-2-6-2015-IP-1, Chemistry, Effluents, and Environmental
        Monitoring Snapshot Self-Assessment, LO-IP3LO-2015-00126, Chemistry-REMP
Section 4OA2: Problem Identification and Resolution
Procedures
EN-DC-204, Maintenance Rule Scope and Basis, Revision 3
EN-DC-204, Maintenance Rule Scope and Basis, Revision 3
EN-DC-207, Maintenance Rule Periodic Assessment, Revision 3


                                            A-10
Apparent Cause Evaluations  
EN-LI-102, Corrective Action Program, Revision 26
IP2-2015-05458  
EN-LI-104, Self-Assessment and Benchmark Process, Revision 11
EN-LI-110-01, Equipment Failure Evaluation, Revision 0
EN-LI-119, Apparent Cause Evaluation Process, Revision 11
EN-OP-104, Operability Determination Process, Revision 10
Condition Reports (CR-IP2)
2010-07013 2015-04574 2015-05458            2015-05460    2015-05461    2015-05464
2015-05466 2015-05467 2016-01374            2016-02348
Condition Reports (CR-IP3)
2015-3628      2016-01035 2016-01961
Maintenance Orders/Work Orders
WO 00442412
Apparent Cause Evaluations
IP2-2015-05458
Drawings
504405, Sheet 1 of 2, Replacement Baffle Bolt Location Matrix, Revision 0
504405, Sheet 2 of 2, Replacement Baffle Bolt Location Matrix, Revision 0
Miscellaneous
61265, Temporary Modification Control Form-Install Additional Temporary Spare Power Supply
      Inside Rod Control Cabinet 2BD to Restore Margin, Revision 0
Appendix A to Facility Operating License DPR-64, Technical Specifications and Basis For The
      Indian Point 3 Nuclear Generating Station Unit No.3, Through Amendment 260
CN-RIDA-15-43, Indian Point Units 2 and 3 Acceptable Baffle-Former Bolting LOCA and
      Seismic Analysis, Revision 2
Engineering Change 63938, As-left condition of the baffle-former plate assembly following the
      replacement of degraded bolts, Revision 0
EPRI TR-112209, Analysis of Baffle Former Bolt Cracking in EDF CPO Plants (PWRMRP-03),
      dated June 1999
Indian Point Entergy Center (IPEC) Unit 3, Updated Final Safety Analysis Report, dated May
      2013
IP-RPT-16-00025, Evaluation of Indian Point Unit 3 Reactor Core Baffle Bolting Following MRP-
      227-A Inspection Findings at Indian Point Unit 2 during 2R22, Revision 0
LO-IP3LO-2015-72
LTR-PL-16-21, Transmittal of Indian Point Unit 3 Final Engineering Evaluations Supporting
      Extent of Condition Review, Revision 0
LTR-RIDA-16-103, Indian Point Unit 2 Baffle Bolting Anti-Clustering Pattern and Margin
      Assessment, Revision 0
LTR-RIDA-16-152, Indian Point Unit 3 Baffle Bolt Leak Before Break Operability Assessment,
      Revision 0
LTR-RIDA-16-60, Indian Point Unit 2 Baffle Bolting One Cycle Replacement Pattern Summary
      Letter, Revision 0
MRP-227-A, Materials Reliability Program: Pressurized Water Reactor Internals Inspection and
      Evaluation Guidelines (ML120170453)
Operation Decision Making Issue Action Plan for IP3 Baffle Bolt Monitoring, dated May 19, 2016
WCAP-15029-NP-A, Westinghouse Methodology for Evaluating the Acceptability of Baffle-
      Former-Barrel Bolting Distributions Under Faulted Load Conditions, Revision 0
      (ML15222A882)


Drawings 504405, Sheet 1 of 2, Replacement Baffle Bolt Location Matrix, Revision 0  
                                              A-11
504405, Sheet 2 of 2, Replacement Baffle Bolt Location Matrix, Revision 0
WCAP-17949-P, Background and Technical Basis Supporting Engineering Flaw Acceptance
      Criteria for Indian Point Unit 2 Reactor Vessel Internals MRP-227-A Primary and
      Expansion Components, Revision 1
WCAP-18048-P, Determination of Acceptable Baffle-Former Bolting for Indian Point Units 2 and
      3, Revision 0
Section 4OA5: Other Activities
Miscellaneous
INPO Letter, INPO Equipment Reliability Scram Review Visit, May 31, 2016
Root Cause Evaluation for CR-IP2-2016-00564


                                A-12
Miscellaneous 61265, Temporary Modification Control Form-Install Additional Temporary Spare Power Supply Inside Rod Control Cabinet 2BD to Restore Margin, Revision 0 Appendix A to Facility Operating License DPR-64, Technical Specifications and Basis For The Indian Point 3 Nuclear Generating Station Unit No.3, Through Amendment 260 CN-RIDA-15-43, Indian Point Units 2 and 3 Acceptable Baffle-Former Bolting LOCA and
                      LIST OF ACRONYMS
Seismic Analysis, Revision 2 Engineering Change 63938,  As-left condition of the baffle-former plate assembly following the replacement of degraded bolts, Revision 0 EPRI TR-112209, Analysis of Baffle Former Bolt Cracking in EDF CPO Plants (PWRMRP-03), dated June 1999 Indian Point Entergy Center (IPEC) Unit 3, Updated Final Safety Analysis Report, dated May
10 CFR Title 10 of the Code of Federal Regulations
2013 IP-RPT-16-00025, Evaluation of Indian Point Unit 3 Reactor Core Baffle Bolting Following MRP-227-A Inspection Findings at Indian Point Unit 2 during 2R22, Revision 0 LO-IP3LO-2015-72
ADAMS Agencywide Document Access and Management System
LTR-PL-16-21, Transmittal of Indian Point Unit 3 Final Engineering Evaluations Supporting Extent of Condition Review, Revision 0 LTR-RIDA-16-103, Indian Point Unit 2 Baffle Bolting Anti-Clustering Pattern and Margin Assessment, Revision 0 LTR-RIDA-16-152, Indian Point Unit 3 Baffle Bolt Leak Before Break Operability Assessment, Revision 0 LTR-RIDA-16-60, Indian Point Unit 2 Baffle Bolting One Cycle Replacement Pattern Summary Letter, Revision 0 MRP-227-A, Materials Reliability Program: Pressurized Water Reactor Internals Inspection and Evaluation Guidelines (ML120170453) Operation Decision Making Issue Action Plan for IP3 Baffle Bolt Monitoring, dated May 19, 2016
ALARA as low as is reasonably achievable
WCAP-15029-NP-A, Westinghouse Methodology for Evaluating the Acceptability of Baffle-Former-Barrel Bolting Distributions Under Faulted Load Conditions, Revision 0 (ML15222A882) 
AVR   automatic voltage regulator
A-11  WCAP-17949-P, Background and Technical Basis Supporting Engineering Flaw Acceptance Criteria for Indian Point Unit 2 Reactor Vessel Internals MRP-227-A Primary and
CAP   corrective action program
Expansion Components, Revision 1 WCAP-18048-P, Determination of Acceptable Baffle-Former Bolting for Indian Point Units 2 and
CCW   component cooling water
3, Revision 0
CR     condition report
Section 4OA5:  Other Activities
CVCS   chemical and volume control system
EC     engineering change
Miscellaneous
ECCS   emergency core cooling system
INPO Letter, INPO Equipment Reliabilit
EDG   emergency diesel generator
y Scram Review Visit, May 31, 2016  Root Cause Evaluation for CR-IP2-2016-00564 
GPI   groundwater protection initiative
A-12  LIST OF ACRONYMS
IASCC irradiation-assisted stress-corrosion cracking
  10 CFR Title 10 of the  
IMC   Inspection Manual Chapter
Code of Federal Regulations ADAMS Agencywide Document Access and Management System ALARA as low as is reasonably achievable  
INPO   Institute of Nuclear Power Operations
AVR automatic voltage regulator  
LER   licensee event report
CAP corrective action program  
LOCA   loss-of-coolant accident
CCW component cooling water  
MBFP   main boiler feedwater pump
CR condition report
MCC   motor control center
CVCS chemical and volume control system EC engineering change  
MOV   motor operated valve
ECCS emergency core cooling system  
MRP   materials reliability program
EDG emergency diesel generator  
MW     monitoring well
GPI groundwater protection initiative IASCC irradiation-assisted stress-corrosion cracking IMC Inspection Manual Chapter  
NCV   non-cited violation
INPO Institute of Nuclear Power Operations  
NRC   Nuclear Regulatory Commission, U.S.
LER licensee event report  
ODCM   offsite dose calculation manual
LOCA loss-of-coolant accident MBFP main boiler feedwater pump MCC motor control center  
OOS   out of service
MOV motor operated valve  
PAB   primary auxiliary building
MRP materials reliability program  
PFP   pre-fire plan
MW monitoring well  
RCS   reactor coolant system
NCV non-cited violation NRC Nuclear Regulatory Commission, U.S. ODCM offsite dose calculation manual  
REMP   radiological environmental monitoring program
OOS out of service  
RFO   refueling outage
PAB primary auxiliary building  
RW     recovery well
PFP pre-fire plan RCS reactor coolant system REMP radiological environmental monitoring program  
SI     safety injection
RFO refueling outage  
SSC   structure, system, and component
RW recovery well  
TS     technical specification
SI safety injection  
UFSAR updated final safety evaluation report
SSC structure, system, and component TS technical specification UFSAR updated final safety evaluation report  
URI   unresolved item
URI unresolved item  
UT     ultrasonic testing
UT ultrasonic testing  
WO     work order
WO work order
}}
}}

Revision as of 14:41, 30 October 2019

Integrated Inspection Report 05000247/2016002 and 05000286/2016002, April 1, 2016, Through June 30, 2016
ML16243A245
Person / Time
Site: Indian Point  Entergy icon.png
Issue date: 08/30/2016
From: Glenn Dentel
Reactor Projects Branch 2
To: Vitale A
Entergy Nuclear Operations
References
IR 2016002
Download: ML16243A245 (54)


See also: IR 05000247/2016002

Text

UNITED STATES

NUCLEAR REGULATORY COMMISSION

REGION I

2100 RENAISSANCE BLVD.

KING OF PRUSSIA, PA 19406-2713

August 30, 2016

Mr. Anthony J. Vitale

Site Vice President

Entergy Nuclear Operations, Inc.

Indian Point Energy Center

450 Broadway, GSB

P.O. Box 249

Buchanan, NY 10511-0249

SUBJECT: INDIAN POINT NUCLEAR GENERATING - INTEGRATED INSPECTION

REPORT 05000247/2016002 AND 05000286/2016002

Dear Mr. Vitale:

On June 30, 2016, the U.S. Nuclear Regulatory Commission (NRC) completed an inspection at

your Indian Point Nuclear Generating (Indian Point), Units 2 and 3. The enclosed inspection

report documents the inspection results, which were discussed on August 4, 2016, with Larry

Coyle and other members of your staff. Based on additional information provided, the

inspectors conducted an updated exit meeting on August 30, 2016 with John Kirkpatrick, Plant

Operations General Manager and other members of your staff.

The inspection examined activities conducted under your license as they relate to safety and

compliance with the Commissions rules and regulations and with the conditions of your license.

The inspectors reviewed selected procedures and records, observed activities, and interviewed

personnel.

This report documents three NRC-identified findings of very low safety significance (Green).

These findings involved violations of NRC requirements. However, because of the very low

safety significance, and because they are entered into your corrective action program, the NRC

is treating these findings as non-cited violations, consistent with Section 2.3.2.a of the NRC

Enforcement Policy. If you contest any non-cited violation in this report, you should provide a

response within 30 days of the date of this inspection report, with the basis for your denial, to

the Nuclear Regulatory Commission, ATTN: Document Control Desk, Washington, DC

20555-0001; with copies to the Regional Administrator, Region I; the Director, Office of

Enforcement, U.S. Nuclear Regulatory Commission, Washington, DC 20555-0001; and the

NRC Senior Resident Inspector at Indian Point. In addition, if you disagree with the

cross-cutting aspect assigned to any finding in this report, you should provide a response within

30 days of the date of this inspection report, with the basis for your disagreement, to the

Regional Administrator, Region I, and the NRC Senior Resident Inspector at Indian Point.

A. Vitale -2-

In accordance with Title 10 of the Code of Federal Regulations (10 CFR) 2.390 of the NRCs

Rules of Practice, a copy of this letter, its enclosure, and your response (if any) will be

available electronically for public inspection in the NRCs Public Document Room or from the

Publicly Available Records component of the NRCs Agencywide Documents Access and

Management System (ADAMS). ADAMS is accessible from the NRC website at

http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room).

Sincerely,

/RA/

Glenn T. Dentel, Chief

Reactor Projects Branch 2

Division of Reactor Projects

Docket Nos. 50-247 and 50-286

License Nos. DPR-26 and DPR-64

Enclosure:

Inspection Report 05000247/2016002 and 05000286/2016002

w/Attachment: Supplementary Information

cc w/encl: Distribution via ListServ

ML16243A245

Non-Sensitive Publicly Available

SUNSI Review

Sensitive Non-Publicly Available

OFFICE RI/DRP RI/DRP RI/DRS RI/DRP RI/DRP

BHaagensen/bh

NAME NFloyd/nf MGray/mg GDentel/gtd MScott/dlp for

DATE 8/29/16 8/24/16 8/30/16 8/30/16 8/30/16

1

U.S. NUCLEAR REGULATORY COMMISSION

REGION I

Docket Nos. 50-247 and 50-286

License Nos. DPR-26 and DPR-64

Report Nos. 05000247/2016002 and 05000286/2016002

Licensee: Entergy Nuclear Northeast (Entergy)

Facility: Indian Point Nuclear Generating Units 2 and 3

Location: 450 Broadway, GSB

Buchanan, NY 10511-0249

Dates: April 1, 2016, through June 30, 2016

Inspectors: B. Haagensen, Senior Resident Inspector

G. Newman, Resident Inspector

S. Rich, Resident Inspector

S. Galbreath, Reactor Inspector

J. Furia, Senior Health Physicist

N. Floyd, Senior Project Engineer

K. Mangan, Senior Reactor Inspector

J. Poehler, Senior Materials Engineer

Approved By: Glenn T. Dentel, Chief

Reactor Projects Branch 2

Division of Reactor Projects

Enclosure

2

TABLE OF CONTENTS

SUMMARY .................................................................................................................................... 3

REPORT DETAILS ....................................................................................................................... 5

1. REACTOR SAFETY .............................................................................................................. 5

1R04 Equipment Alignment .................................................................................................. 5

1R05 Fire Protection ............................................................................................................. 6

1R07 Heat Sink Performance ............................................................................................... 7

1R08 Inservice Inspection Activities ..................................................................................... 7

1R11 Licensed Operator Requalification Program ............................................................... 8

1R12 Maintenance Effectiveness ....................................................................................... 10

1R13 Maintenance Risk Assessments and Emergent Work Control .................................. 13

1R15 Operability Determinations and Functionality Assessments ..................................... 14

1R18 Plant Modifications .................................................................................................... 19

1R19 Post-Maintenance Testing ........................................................................................ 20

1R20 Refueling and Other Outage Activities ...................................................................... 21

1R22 Surveillance Testing .................................................................................................. 24

1EP6 Drill Evaluation .......................................................................................................... 25

2. RADIATION SAFETY .......................................................................................................... 25

2RS1 Radiological Hazard Assessment and Exposure Controls ........................................ 25

2RS2 Occupational As Low As Is Reasonably Achievable (ALARA) Planning

and Controls .............................................................................................................. 26

2RS7 Radiological Environmental Monitoring Program (REMP) ........................................ 26

4. OTHER ACTIVITIES ............................................................................................................ 27

4OA1 Performance Indicator Verification ............................................................................ 27

4OA2 Problem Identification and Resolution ....................................................................... 28

4OA3 Follow Up of Events and Notices of Enforcement Discretion .................................... 34

4OA5 Other Activities .......................................................................................................... 37

4OA6 Meetings, Including Exit ............................................................................................ 39

SUPPLEMENTARY INFORMATION ........................................................................................ A-1

KEY POINTS OF CONTACT .................................................................................................... A-1

LIST OF ITEMS OPENED, CLOSED, DISCUSSED, AND UPDATED ..................................... A-2

LIST OF DOCUMENTS REVIEWED ........................................................................................ A-3

LIST OF ACRONYMS ............................................................................................................. A-12

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SUMMARY

Inspection Report 05000247/2016002 and 05000286/2016002; 04/01/2016 - 06/30/2016; Indian

Point Nuclear Generating (Indian Point), Units 2 and 3; Operability Determinations and

Functionality Assessments, Refueling and Other Outage Activities, and Follow Up of Events and

Notices of Enforcement Discretion.

This report covered a three-month period of inspection by resident inspectors and announced

inspections performed by regional inspectors. The inspectors identified three findings of very

low safety significance (Green), which were non-cited violations (NCVs). The significance of

most findings is indicated by their color (i.e., greater than Green, or Green, White, Yellow, Red)

and determined using Inspection Manual Chapter (IMC) 0609, Significance Determination

Process, dated April 29, 2015. Cross-cutting aspects are determined using IMC 0310,

Aspects within the Cross-Cutting Areas, dated December 4, 2014. All violations of

U.S. Nuclear Regulatory Commission (NRC) requirements are dispositioned in accordance with

the NRCs Enforcement Policy, dated February 4, 2015. The NRCs program for overseeing the

safe operation of commercial nuclear power reactors is described in NUREG-1649, Reactor

Oversight Process, Revision 6.

Cornerstone: Mitigating Systems

Green. The inspectors identified a Green NCV of 10 CFR 50, Appendix B, Criterion V,

"Instructions, Procedures, and Drawings," because Entergy did not adequately accomplish

the actions prescribed by procedure EN-OP-104, Operability Determination Process, for a

degraded condition associated with the Unit 3 baffle-former bolts. Specifically, Entergy

incorrectly concluded that no degraded or non-conforming condition existed related to the

Unit 3 baffle-former bolts and exited the operability determination procedure. Entergy

subsequently performed the remaining steps in the procedure and provided appropriate

justification for their plans to examine the baffle-former bolts at the next Unit 3 refueling

outage (RFO). Entergys immediate corrective actions included entering the issue into its

corrective action program (CAP) as CR-IP3-2016-01961 and documenting an operability

evaluation to support the basis for operability of the baffle-former bolts and the emergency

core cooling system (ECCS).

This performance deficiency is more than minor because it was associated with the

equipment performance attribute of the Mitigating Systems cornerstone and affected the

cornerstone objective to ensure the availability, reliability, and capability of systems that

respond to initiating events to prevent undesirable consequences (i.e., core damage). In

accordance with IMC 0609.04, Initial Characterization of Findings, and Exhibit 2 of

IMC 0609, Appendix A, The Significance Determination Process for Findings At-Power,

issued June 19, 2012, the inspectors screened the finding for safety significance and

determined it to be of very low safety significance (Green), because the finding did not

represent an actual loss of system or function. After inspector questioning, Entergy

performed an operability evaluation, which provided sufficient bases to conclude the Unit 3

baffle assembly would support ECCS operability. This finding is related to the cross-cutting

aspect of Problem Identification and Resolution, Operating Experience, because Entergy did

not effectively evaluate relevant internal and external operating experience. Specifically,

Entergy did not adequately evaluate the impact of degraded baffle bolts at Unit 3 when

relevant operating experience was identified at Unit 2. [P.5 - Operating Experience]

(Section 1R15)

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Green. The inspectors identified a Green NCV of Technical Specification (TS) 5.4.1,

Procedures, for Entergys failure to implement procedure OAP-007, Containment Entry

and Egress. Specifically, workers transiting the inner and outer crane wall sections of

containment failed to maintain at least one (of two) flow channeling gate closed to ensure

availability of the containment sumps to provide suction for the ECCS. Entergy immediately

coached the gate monitor and restored the gates to an acceptable position. Entergy

generated CR-IP2-2016-04036 to address this issue.

This performance deficiency is more than minor because it was associated with the

configuration control (shutdown equipment lineup) attribute of the Mitigating Systems

cornerstone and affected the cornerstone objective to ensure the availability, reliability, and

capability of systems that respond to initiating events to prevent undesirable consequences

(i.e., core damage). A detailed risk assessment was conducted and determined that the

change in core damage frequency was determined to be 7E-9, therefore, this issue

represents a Green finding. This finding had a cross-cutting aspect in the area of Human

Performance, Avoid Complacency, because Entergy did not consider potential undesired

consequences of actions before performing work and implement appropriate error-reduction

tools. Specifically, the work crew did not understand the requirements and potential

consequences prior to commencing work and the gate monitor did not enforce these

requirements to maintain at least one gate locked or pinned closed as required by OAP-007.

[H.12 - Avoid Complacency] (Section 1R20)

Cornerstone: Barrier Integrity

Green. The inspectors identified a Green NCV of 10 CFR 50.65(b)(1) for Entergys failure to

include a function of a safety-related system within the scope of the maintenance rule

program. Specifically, Entergy failed to include the feedwater isolation function performed

by the main boiler feedwater pumps (MBFPs) discharge valves, MBFPs, and feedwater

regulating valves, which are required to remain functional during and following a design

basis event to mitigate the consequence of the accident within the scope of the maintenance

rule monitoring program. Entergy initiated corrective actions to include the feedwater

isolation function performed by the MBFP discharge valves, MBFPs, and feedwater

regulating valves within the maintenance rule monitoring program. Entergy entered this

issue into the CAP as CR-IP2-2016-03963.

This performance deficiency is more than minor because it was associated with barrier

performance attribute of the Barrier Integrity cornerstone and adversely affected the

cornerstone objective to provide reasonable assurance that physical design barriers protect

the public from radionuclide releases caused by accidents or events. Specifically, the failure

to properly scope the feedwater isolation function prevented Entergy from identifying that

equipment reliability was no longer effectively controlled through preventive maintenance.

In accordance with IMC 0609.04, Initial Characterization of Findings, and Exhibit 2 of IMC 0609, Appendix A, The Significance Determination Process for Findings At-Power, issued

June 19, 2012, the inspectors determined that the finding was of very low safety significance

(Green) because the finding did not represent an actual open pathway in the physical

integrity of reactor containment, containment isolation system, and heat removal

components. This finding does not have a cross-cutting aspect since the failure to scope

this equipment into the maintenance rule program was not recognized when Entergy

combined the maintenance rule basis documents for Units 2 and 3 in 2012 and, as a result,

is not indicative of current licensee performance. (Section 4OA3)

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REPORT DETAILS

Summary of Plant Status

Unit 2 began the inspection period during RFO 2R22 which lasted 102 days. Upon completion

of the outage, the operators restarted Unit 2 on June 14, 2016, and increased power slowly to

93 percent for fuel preconditioning. On June 23, 2016, the operators shutdown the reactor to

repair a service water leak on the 21 component cooling water (CCW) heat exchanger (Hx) inlet

line and replace switchyard breaker 9. Unit 2 returned to 100 percent power on June 29, 2016.

Unit 2 remained at or near 100 percent power for the remainder of the inspection period.

Unit 3 began the inspection period at 100 percent power. On April 26, 2016, a failed controller

caused both heater drain pumps to trip; and the operators reduced power rapidly, stabilizing the

unit at 48 percent power. Operators returned Unit 3 to 100 percent power on April 27, 2016,

and remained at or near 100 percent power for the remainder of the inspection period.

1. REACTOR SAFETY

Cornerstones: Initiating Events, Mitigating Systems, and Barrier Integrity

1R04 Equipment Alignment

Partial System Walkdowns (71111.04Q - 5 samples)

a. Inspection Scope

The inspectors performed partial walkdowns of the following systems:

Unit 2

Spent fuel pool cooling system following core offload on May 19, 2016

Shutdown cooling system following core reload on June 6, 2016

CCW system following maintenance on June 28, 2016

Unit 3

32 emergency diesel generator (EDG) following maintenance on May 9, 2016 (this

sample was part of an in-depth review of the EDG system)

Residual heat removal pumps following CCW system testing on May 20, 2016

The inspectors selected these systems based on their risk-significance relative to the

reactor safety cornerstones at the time they were inspected. The inspectors reviewed

applicable operating procedures, system diagrams, the updated final safety analysis

report (UFSAR), TSs, work orders (WOs), condition reports (CRs), and the impact of

ongoing work activities on redundant trains of equipment in order to identify conditions

that could have impacted system performance of their intended safety functions. The

inspectors also performed field walkdowns of accessible portions of the systems to verify

system components and support equipment were aligned correctly and were operable.

The inspectors examined the material condition of the components and observed

operating parameters of equipment to verify that there were no deficiencies. The

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inspectors also reviewed whether Entergy had properly identified equipment issues and

entered them into the CAP for resolution with the appropriate significance

characterization. Documents reviewed for each section of this inspection report are

listed in the Attachment.

b. Findings

No findings were identified.

1R05 Fire Protection

Resident Inspector Quarterly Walkdowns (71111.05Q - 6 samples)

a. Inspection Scope

The inspectors conducted tours of the areas listed below to assess the material

condition and operational status of fire protection features. The inspectors verified that

Entergy controlled combustible materials and ignition sources in accordance with

administrative procedures. The inspectors verified that fire protection and suppression

equipment were available for use as specified in the area pre-fire plan (PFP) and

passive fire barriers were maintained in good material condition. The inspectors also

verified that station personnel implemented compensatory measures for out-of-service

(OOS), degraded, or inoperable fire protection equipment, as applicable, in accordance

with procedures.

Unit 2

Containment, 95-foot elevation, during baffle bolt repair activities with hot work in

progress (PFP-203 was reviewed) on June 2, 2016

Residual heat removal pump rooms in primary auxiliary building (PAB), 15-foot

elevation (PFP-204 was reviewed), on June 6, 2016

CCW pump room, 68-foot elevation (PFP-209 was reviewed), on June 25, 2016

PAB, 80-foot elevation, CCW heat exchanger area with hot work in progress

(PFP-211 was reviewed) on June 25, 2016

Unit 3

32 EDG room, 10-foot elevation (PFP-354 was reviewed), on May 9, 2016

480V switchgear room, 15-foot elevation (PFP-351 was reviewed), on June 30, 2016

b. Findings

No findings were identified.

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1R07 Heat Sink Performance (71111.07A - 1 sample)

a. Inspection Scope

The inspectors reviewed the 32 EDG jacket water and lube oil heat exchanger to

determine its readiness and availability to perform its safety functions. The inspectors

reviewed the design basis for the component and verified Entergys commitments to

NRC Generic Letter 89-13, Service Water System Requirements Affecting

Safety-Related Equipment. The inspectors observed the annual cleaning and

inspection of the heat exchangers and reviewed the results of previous inspections of

the Unit 3 EDG heat exchangers. The inspectors discussed the results of the most

recent inspection with engineering staff. The inspectors verified that Entergy initiated

appropriate corrective actions for identified deficiencies. The inspectors also verified

that the number of tubes plugged within the heat exchanger did not exceed the

maximum amount allowed.

b. Findings

No findings were identified.

1R08 Inservice Inspection Activities (71111.08P - 1 sample)

a. Inspection Scope

Inspectors from the NRC Region I Office, specializing in materials and inservice

examination activities, observed portions of Entergys activities involving baffle-former

bolt examinations and replacements during Unit 2 RFO 2R22. The inspectors reviewed

work documentation and examination procedures and results, and discussed these

activities with Entergy. The inspectors were on-site from April 27 to April 28, 2016, and

on May 23, 2016. The inspectors verified that Entergy completed baffle-former bolt

examinations in accordance with their approved procedures which implemented

activities described in the Materials Reliability Program (MRP)-227-A, Pressurized

Water Reactor Internals Inspection and Evaluation Guidelines, as they relate to this

component. Specifically, the inspectors reviewed the results of the visual and volumetric

examinations of the baffle-former bolts, including capabilities, limitations, and

acceptance criteria that were performed during the current RFO.

Non-Destructive Examination Activities

The inspectors reviewed the ultrasonic testing (UT) procedure used for the examination

of the Unit 2 baffle-former bolts to verify the procedure was in accordance with the

applicable guidance in MRP-227-A and MRP-228. The inspectors reviewed the UT data

records and the detailed UT channel analysis for a sample of baffle-former bolts to verify

the examinations and evaluations were performed in accordance with approved

procedures and applicable guidance. The inspectors reviewed video recordings of the

visual examinations of the baffle-former bolts during the current RFO. The inspectors

also reviewed recorded video of visual examinations performed in 2006 at Unit 2,

completed as part of the existing inservice inspection program for the 10-year reactor

vessel examinations, to independently assess the past conditions of the baffle-former

bolts and assembly.

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The inspectors reviewed certifications of the UT technicians performing the ultrasonic

examinations to verify the examinations were performed by qualified individuals and to

verify the results were reviewed and evaluated by certified level III non-destructive

examination personnel.

Baffle-Former Bolt Replacement Activities

The inspectors reviewed the baffle-former bolt replacement activities performed as part

of a corrective action to resolve the degraded condition identified at Unit 2. The

inspectors observed a sample of in-process bolt removal activities, which included lock

bar milling and bolt hole machining. The inspectors reviewed the documentation for

in-process and completed bolt installation activities and verified that loose parts

generated as part of the bolt replacements were properly tracked. The inspectors

verified that bolt replacement activities were performed in accordance with approved

procedures. The inspectors also reviewed the Engineering Change (EC) package

associated with the new baffle-former bolt design. This review is documented in

Section 1R18 of this report. After completion of the bolt replacement activities, the

inspectors reviewed the video of the final visual examination of the baffle assembly to

verify that the baffle-former bolt work was accomplished as planned and that there were

no visual indications of deficiencies.

b. Findings

No findings were identified.

Update to URI 05000247/2016001-01, Baffle-Former Bolts with Identified Anomalies

This inspection was conducted to follow-up on NRC Unresolved Item (URI)05000247/2016001-01, Baffle-Former Bolts with Identified Anomalies, to determine

whether there was a performance deficiency associated with the degraded baffle-former

bolt condition discovered at Unit 2. The inspectors plan to review additional technical

information from Entergy as it becomes available, including any revisions to the root

cause evaluation. The URI remains open until review of this additional information is

completed. (URI 05000247/2016001-01, Baffle-Former Bolts with Identified

Anomalies)

1R11 Licensed Operator Requalification Program (71111.11Q - 5 samples)

Unit 2

.1 Quarterly Review of Unit 2 Licensed Operator Requalification Testing and Training

(71111.11Q - 1 sample)

a. Inspection Scope

The inspectors observed Unit 2 licensed operator simulator training on May 24, 2016,

which included reactor coolant pump seal failure with loss of normal heat sink requiring

implementation of feed and bleed cooling. The inspectors evaluated operator

performance during the simulated event and verified completion of risk significant

operator actions, including the use of abnormal and emergency operating procedures.

The inspectors assessed the clarity and effectiveness of communications,

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implementation of actions in response to alarms and degrading plant conditions, and the

oversight and direction provided by the control room supervisor. The inspectors verified

the accuracy and timeliness of the emergency classification made by the shift manager

and the TS action statements entered by the shift technical advisor. Additionally, the

inspectors assessed the ability of the crew and training staff to identify and document

crew performance problems.

b. Findings

No findings were identified.

.2 Quarterly Review of Unit 3 Licensed Operator Requalification Testing and Training

(71111.11Q - 1 sample)

a. Inspection Scope

The inspectors observed a Unit 3 licensed operator simulator requalification training

evaluated scenario on May 24, 2016, which included failure of a pressurizer pressure

instrument, charging pump trip, loss of 480V safety bus 5A, a small break loss-of-coolant

accident (LOCA), and entry into FR-C.2 core cooling. The inspectors evaluated operator

performance during the simulated event and verified completion of risk significant

operator actions, including the use of abnormal and emergency operating procedures.

The inspectors assessed the clarity and effectiveness of communications,

implementation of actions in response to alarms and degrading plant conditions, and the

oversight and direction provided by the control room supervisor. The inspectors verified

the accuracy and timeliness of the emergency classification made by the shift manager

and the TS action statements entered by the shift technical advisor. Additionally, the

inspectors assessed the ability of the crew and training staff to identify and document

crew performance problems.

b. Findings

No findings were identified.

.3 Quarterly Review of Licensed Operator Performance (71111.11Q - 3 samples)

a. Inspection Scope

The inspectors conducted a focused observation of operator performance in the main

control room. The inspectors observed pre-job briefings and control room

communications to verify they met the criteria specified in Entergys administrative

procedure EN-OP-115, Conduct of Operations. Additionally, the inspectors observed

restoration activities to verify that procedure use, crew communications, and

coordination of activities between work groups similarly met established expectations

and standards.

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Unit 2

Plant startup from RFO 2R22 on June 16, 2016 including response to a turbine trip

without a reactor trip and the subsequent turbine-generator synchronization and

transfer of plant electrical loads from offsite power to the unit auxiliary transformer.

Reactor startup and grid synchronization conducted on June 27, 2016.

Unit 3

Operator response to the feedwater transient which occurred on April 26, 2016

b. Findings

No findings were identified.

1R12 Maintenance Effectiveness (71111.12Q - 4 samples)

.1 Routine Maintenance Effectiveness

a. Inspection Scope

The inspectors reviewed the samples listed below to assess the effectiveness of

maintenance activities on SSCs performance and reliability. The inspectors reviewed

system health reports, CAP documents, maintenance WOs, and maintenance rule basis

documents to ensure that Entergy was identifying and properly evaluating performance

problems within the scope of the maintenance rule. For each SSC sample selected, the

inspectors verified that the SSC was properly scoped into the maintenance rule in

accordance with 10 CFR 50.65 and verified that the (a)(2) performance criteria

established by Entergy was reasonable. As applicable, for SSCs classified as (a)(1), the

inspectors assessed the adequacy of goals and corrective actions to return these SSCs

to (a)(2). Additionally, the inspectors ensured that Entergy was identifying and

addressing common cause failures that occurred within and across maintenance rule

system boundaries.

Unit 2 EDGs

Unit 3 EDGs (this sample was part of an in-depth review of the EDG system)

Units 2 and 3 CVCS

b. Findings

No findings were identified.

URI Opened, CVCS Goal Monitoring Under the Maintenance Rule

Introduction

The inspectors identified issues of potential concern with Entergys application of

10 CFR 50.65(a)(1), Requirements for Monitoring the Effectiveness of Maintenance at

Nuclear Plants, (the maintenance rule) in regards to the reliability of the Unit 2 CVCS

system. These concerns included the establishment of appropriate (a)(1) goals and

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whether appropriate justification was established that the corrective actions to address

identified maintenance weaknesses were effective prior to removal from (a)(1) status.

Specifically, Entergy may have established restrictive goals without defensible

justification and may not have demonstrated their chosen goal before ending the goal

monitoring interval.

Description

The maintenance rule requires that licensees shall monitor the performance or condition

of structures, systems, or components, against licensee-established goals, in a manner

sufficient to provide reasonable assurance that these structures, systems, and

components are capable of fulfilling their intended functions. These goals shall be

established commensurate with safety and, where practical, take into account

industrywide operating experience. When the performance or condition of a structure,

system, or component does not meet established goals, appropriate corrective action

shall be taken. EN-DC-206, Maintenance Rule (a)(1) Process, provides the

requirements and processes for managing SSCs for which (a)(2) monitoring has not

demonstrated effective maintenance. EN-DC-206 specifies that (a)(1) action plans

should not be closed until effectiveness of all corrective actions has been demonstrated

by meeting performance goals through the monitoring period (or by other means

specified in the action plan).

Since 2013, there have been several repeat functional failures of equipment in the

CVCS resulting in a failure to meet the performance criterion for reliability. These

failures included:

A failure of the 23 charging pump on August 6, 2013, after the internal oil pump

discharge tubing broke causing the pump to trip on low oil pressure and a loss of

charging. The 21 charging pump had tripped for the same reason in 2010.

A failure of the 22 charging pump on January 14, 2014, due to cracked internal

check valves caused by an inadequate fill-and-vent that left air in the pump following

maintenance. The 21 charging pump had failed due to the same cause in 2013.

A failure of the Unit 2 valve FCV-110A, boric acid flow control valve, to fully open on

January 5, 2015. The valve had insufficient insulation; and as a result, boron

crystalized above the valve plug and blocked its movement. The Unit 3 FCV-110A

had failed in the same way in 2011, with earlier failures of other valves for the same

cause going back to 1997.

In each case, the CVCS for Unit 2 was already (a)(1), so Entergy either updated the

existing (a)(1) action plan or created another one to operate in parallel with the existing

one. Upon reviewing the associated (a)(1) action plans, the inspectors noted that in

each example Entergys goals may not have been in accordance with EN-DC-206(a)(1)

Process. It specifies that monitoring intervals should be at least six months for normally

operating SSCs, at least three surveillances for SSCs monitored by surveillance and

long enough to detect recurrence of the applicable failure mechanism. It also states that

performance goals that provide reasonable assurance that the SSC is capable of

performing its intended functions should be monitored throughout the time the SSC is

classified (a)(1). EN-DC-206 defines an SSC as any discreet component grouping that

has caused a monitoring failure, including any applicable extent of condition. In the

examples provided, NRC inspectors challenged whether Entergy either chose a shorter

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monitoring interval or a goal that did not include the applicable extent of condition.

Specifically:

The (a)(1) action plan for the broken oil tubing had a goal of no noticeable decrease

in 23 charging pumps running oil pressure for the next three quarterly surveillances.

The chosen monitoring interval met the procedural expectation, but Entergy limited

the monitoring to the 23 charging pump without written justification, when the 21

charging pump had failed previously for the same reason and the other pumps were

susceptible to the same failure mechanism. During the monitoring interval, the 21

charging pump experienced low oil pressure. When Entergy performed repairs on

the 21 charging pump for an unrelated issue, they discovered that the oil tubing had

failed in the same way the 23 charging pump oil tubing had failed, although it had not

yet caused a pump trip.

The (a)(1) action plan for the cracked check valves had a goal of no check valve

failure for six months for the next charging pump that underwent maintenance. This

happened to be the 22 charging pump. Entergy chose a six-month monitoring

interval, even though only one of the three charging pumps is in service at any given

time, and the 22 charging pump only ran for four out of the six months it was

monitored. Additionally, the action plan did not justify why a single successful fill-

and-vent demonstrated adequate corrective actions. On November 19, 2014, during

the six month monitoring interval, the 21 charging pump underwent maintenance

requiring a fill-and-vent, and experienced check valve failure two weeks later on

December 4. Entergy documented this as a maintenance rule functional failure, and

discussed the possibility that it could be due to an inadequate fill-and-vent, but did

not change the (a)(1) action plan.

The (a)(1) action plan for FCV-110A specified a monitoring interval of six months to

include the winter because the previous valve failures had all occurred during the

winter months. However, the actual monitoring interval documented in the corrective

action was from April to October 2015, and therefore did not cover the winter months

as intended. In January 2016, Entergy performed maintenance on valve CH-297 on

Unit 3, which is a heat-traced boric acid valve, and did not properly restore the

insulation. The valve function was not impacted because it does not often contain

high concentrations of boric acid.

The (a)(1) action plans described above were all reviewed and approved by the

maintenance rule expert panel.

Further information regarding the performance of these SSCs is required to determine

whether these issues of concern represent performance deficiencies and whether they

are more than minor. (URI 05000247/2016002-01, CVCS Goal Monitoring Under the

Maintenance Rule)

.2 Quality Control

a. Inspection Scope

The inspectors reviewed the weld repair performed on the 21 CCW heat exchanger

service water inlet nozzle for Unit 2 to verify Entergy was properly applying quality

controls specified in their quality assurance program. The inspectors reviewed CAP

documents, maintenance WOs, ECs, and engineering procedures associated with the

weld repair. The inspectors verified Entergy specified quality control hold points in

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accordance with their procedures, properly controlled the quality of materials used

during the repair, and adequately justified deviations from the existing design.

Additionally, the inspectors reviewed the welding procedure specification qualification by

the vendor to ensure it was in accordance with American Society of Mechanical

Engineers code.

b. Findings

No findings were identified.

1R13 Maintenance Risk Assessments and Emergent Work Control (71111.13 - 7 samples)

a. Inspection Scope

The inspectors reviewed station evaluation and management of plant risk for the

maintenance and emergent work activities listed below to verify that Entergy performed

the appropriate risk assessments prior to removing equipment for work. The inspectors

selected these activities based on potential risk significance relative to the reactor safety

cornerstones. As applicable for each activity, the inspectors verified that Entergy

performed risk assessments as required by 10 CFR 50.65(a)(4) and that the

assessments were accurate and complete. When Entergy performed emergent work,

the inspectors verified that operations personnel promptly assessed and managed plant

risk. The inspectors reviewed the scope of maintenance work and discussed the results

of the assessment with the stations probabilistic risk analyst to verify plant conditions

were consistent with the risk assessment. The inspectors also reviewed the TS

requirements and inspected portions of redundant safety systems, when applicable, to

verify risk analysis assumptions were valid and applicable requirements were met.

Unit 2

Temporary loss of spent fuel pool cooling due to 345-kilovolt disturbance on

April 3, 2016

Equipment hatch closure plug seal demonstration for outage risk on April 5, 2016

Reduced inventory operations during vessel reassembly on June 7, 2016

21 CCW heat exchanger OOS during mode 4 on June 25, 2016

Unit 3

32 EDG OOS while Bus Tie BT 4-5 was OOS on May 4, 2016 (this sample was part

of an in-depth review of the EDG system)

33 EDG OOS while Bus Tie BT 4-5 was OOS on June 2, 2016

31 EDG OOS while Bus Tie BT 4-5 was OOS on June 21, 2016

b. Findings

No findings were identified.

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1R15 Operability Determinations and Functionality Assessments (71111.15 - 7 samples)

a. Inspection Scope

The inspectors reviewed operability determinations for the following degraded or

non-conforming conditions:

Unit 2

23 EDG failure to run on March 7, 2016, and subsequent failure to pass the

surveillance test on March 10, 2016, as identified in CR-IP2-2016-01260

Operability determination for N33 gamma metrics wide range nuclear instrument

channel in CR-IP2-2016-03660 on June 13, 2016

Pressurizer level transmitter LT-461 reads high in CR-IP-2016-3806 on June 14,

2016

Through-wall leak in line 411, service water inlet to the 21 CCW heat exchanger, on

June 15, 2016

Unit 3

Immediate operability determination of the degraded condition of the baffle-former

bolts identified from Unit 2 operating experience in CR-IP3-2016-01035 on April 1,

2016

Anomalies noted during digital metal impact monitoring system self-test in

CR-IP3-2015-03468 on April 1, 2016

Prompt operability determination of the degraded condition of the baffle-former bolts

identified from Unit 2 operating experience in CR-IP2-2016-03660 on June 30, 2016

The inspectors selected these issues based on the risk significance of the associated

components and systems. The inspectors evaluated the technical adequacy of the

operability determinations to assess whether TS operability was properly justified and

the subject component or system remained available such that no unrecognized

increase in risk occurred. The inspectors compared the operability and design criteria in

the appropriate sections of the TSs and UFSAR to Entergys evaluations to determine

whether the components or systems were operable.

The inspectors confirmed, where appropriate, compliance with bounding limitations

associated with the evaluations. Where compensatory measures were required to

maintain operability, the inspectors determined whether the measures in place would

function as intended and were properly controlled by Entergy. The inspectors

determined, where appropriate, compliance with bounding limitations associated with the

evaluations.

b. Findings

Introduction. The inspectors identified a Green NCV of 10 CFR 50, Appendix B,

Criterion V, "Instructions, Procedures, and Drawings," because Entergy did not

adequately accomplish the actions prescribed by procedure EN-OP-104 for a degraded

condition associated with the Unit 3 baffle-former bolts. Specifically, Entergy incorrectly

concluded that no degraded or non-conforming condition existed related to the Unit 3

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baffle-former bolts and exited the operability determination procedure. Entergy

subsequently performed the remaining steps in the procedure and provided appropriate

justification for their plans to examine the baffle-former bolts at the next Unit 3 RFO.

Description. On March 29, 2016, Entergy identified baffle-former (baffle) bolt

degradation at Indian Point Unit 2 that was determined to be unanalyzed because it did

not meet the minimum acceptable bolt pattern analysis developed to support plant

startup. Entergy staff identified a total of 227 baffle bolts out of a population of 832 that

were potentially degraded (182 bolts had UT indications; 31 had visual indications of

failure; and 14 were inaccessible for testing and conservatively assumed to be

degraded). Entergy staff entered this problem into the CAP as CR-IP2-2016-02081,

performed a root cause evaluation, and replaced the degraded bolts on Unit 2. Due to

the number of baffle bolt indications discovered on Unit 2, Entergy staff initiated CR-IP3-

2016-01035 on April 21, 2016, and performed an immediate operability determination

(IOD) in accordance with Entergy procedure EN-OP-104 Section 5.3, to evaluate the

baffle bolts and baffle-former assembly structure on Unit 3. Entergy staff planned further

corrective actions to move up the planned Unit 3 baffle bolt ultrasonic examinations to

the next RFO in spring 2017.

The inspectors reviewed the design basis and current licensing basis documents for

Indian Point Unit 3 to identify the specific safety functions of the baffle bolts. The baffle

bolts are part of the baffle former assembly structure located in the reactor pressure

vessel. The bolts secure a series of vertical metal plates called baffle plates, which help

direct water up through the nuclear fuel assemblies to ensure proper cooling of the fuel.

A sufficient number of baffle bolts are required to secure the plates to ensure proper

core flow during normal and postulated accident conditions, and also to ensure that

control rods can be inserted to shut down the reactor.

The inspectors reviewed Entergys IOD issued on April 21, 2016, and concluded the

immediate determination was completed in accordance with Section 5.3 of procedure

EN-OP-104. The IOD provided sufficient technical detail to support the initial conclusion,

based on limited information, that the Unit 3 baffle bolts would retain sufficient capability

to perform their intended functions. Specifically, the IOD stated that Unit 2 baffle bolt

failures were likely due to irradiation-assisted stress corrosion cracking (IASCC) and that

the Unit 3 baffle bolts were also susceptible because they both utilize a baffle bolt design

with similar geometry and material to other plants with bolt failures. The IOD concluded

that Unit 3 baffle bolt degradation would likely not be as significant as Unit 2, and that

the Unit 3 baffle former assembly was currently operable pending further evaluation

because of the following differences with Unit 2: (1) less effective full power years of

operation; (2) less neutron fluence levels (i.e., irradiation); (3) less pressure differential

across the baffle plates; and (4) less fatigue-induced loading cycles on the bolts over the

operating life of the plant. The inspectors concluded that there was no immediate safety

concern.

On May 5, 2016, Entergy staff revised the operability input for CR-IP3-2016-01035 under

corrective action #2. The inspectors noted that Entergy staff concluded an operability

evaluation was not needed, in part, because the baffle-former bolts are not required by

TS and are not described in the UFSAR. The inspectors noted that while the baffle

bolts are not described in these documents, their failure in sufficient numbers could have

consequential effects on the TS-controlled ECCS if the baffle plates were to become

detached or deformed. This was described in Entergys bolt pattern analysis report

16

documenting an acceptable bolt pattern prior to the spring 2016 RFO. The inspectors

reviewed Unit 3 TS 3.5.2, ECCS - Operating, which requires multiple trains of ECCS to

be operable. The inspectors concluded that since the baffle bolts support the ECCS,

which is subject to TS, Entergys decision to not perform further evaluation of the

operability determination was inconsistent with EN-OP-104. Specifically, Section 5.1(7)

of Entergys procedure EN-OP-104 requires that an operability determination be

performed whenever a condition exists in the supporting SCC that may affect the ability

of the TS-controlled SSC to perform its specified safety function.

Further, the inspectors noted that Entergy staff concluded a degraded condition did not

exist in Unit 3, and therefore, an operability evaluation was not required as a follow-up to

the immediate determination. The documented basis provided was the differences

between the two units, plant operating data, and fuel performance. The inspectors noted

that plant operating data and fuel performance from Unit 2 did not result in identification

of the bolt degradation; therefore, the absence of indications for these problems on Unit

3 was technically insufficient to support Entergys conclusion that there was no degraded

condition on Unit 3.

The inspectors review of procedure EN-OP-104, Section 3.0, identified that examples of

the effects of equipment aging and operating experience can be sources of information

considered to enter the operability or functionality process. The inspectors

acknowledged that licensees apply judgment in these decisions. In this particular

instance, the inspectors considered that operating experience was available that showed

the Unit 3 baffle bolts were subject to IASCC and that plants of similar design (4-loop

Westinghouse pressurized water reactors with a down-flow configuration and baffle bolts

of 347 material and similar dimensions) were subject to greater amounts of bolt

degradation compared to other reactor designs. Furthermore, the inspectors noted the

baffle bolts had experienced levels of neutron radiation exposure above the threshold for

IASCC initiation as referenced in NUREG/CR-7027, Degradation of LWR Core Internal

Materials due to Neutron Irradiation.

Based on the above information available to Entergy staff, the inspectors concluded that

Entergys basis for determining that a degraded condition did not exist on Unit 3 was not

technically supported. The inspectors noted that in completing an IOD in EN-OP-104,

Step 5.3.2 states determine if there is an ongoing degradation mechanism that may

impact future operability based on changing conditions, specifically consider the SSCs

specified safety function and mission time. On May 5, 2016, Entergys basis for

concluding an operability evaluation was not required and exiting the operability

determination procedure at Step 5.3.3 was inconsistent with this procedural requirement

because their IOD concluded Unit 3 was susceptible to baffle bolt degradation, which is

time based and subject to changing conditions including fatigue inducing loading cycles

and neutron fluence. As a result, the inspectors concluded Entergy staff did not

complete the additional actions prescribed by EN-OP-104 to perform an operability

evaluation. Specifically, Step 5.3.9 states in part if an Operability Evaluation is required

then perform the following: Proceed to Subsection 5.5, Operability Evaluation.

On July 11, 2016, Entergy staff subsequently completed the steps in EN-OP-104 and

performed an operability evaluation, which assumed an estimated number of baffle-

former bolt failures based on the degradation found in Unit 2, and adjusted to take credit

for the small number of inaccessible bolts and a sample of bolts extracted with high

removal torque that indicated residual structural capacity. The inspectors determined

17

this estimated number of bolt failures was conservative because the evaluation did not

credit the baffle-edge bolts or the differences in operational history between the two units

such as neutron fluence levels or fatigue from thermal cycles. The operability evaluation

concluded that the Unit 3 baffle bolts would perform as intended to secure the baffle

plates from being dislodged. The inspectors concluded that Entergys operability

evaluation provided appropriate basis to conclude that the Unit 3 baffle assembly would

support ECCS operability until the planned Unit 3 RFO in spring 2017.

Analysis. The inspectors determined that Entergys failure to adequately accomplish the

actions prescribed in EN-OP-104 for a degraded condition and perform an operability

evaluation associated with the Unit 3 baffle-former bolts was a performance deficiency.

Specifically, Entergy incorrectly concluded that no degraded or non-conforming condition

existed related to the Unit 3 baffle-former bolts and exited the operability determination

procedure. As a result, Entergys initial documentation did not provide sufficient basis

for operability and continued operation until questioned by NRC inspectors.

This finding is more than minor because it is associated with the equipment performance

attribute of the Mitigating Systems cornerstone and affected the cornerstone objective to

ensure the availability, reliability, and capability of systems that respond to initiating

events to prevent undesirable consequences (i.e., core damage). This issue was also

similar to example 3.j of IMC 0612, Appendix E, Examples of Minor Issues, because

the condition resulted in reasonable doubt of operability of the ECCS and additional

analysis was necessary to verify operability. In accordance with IMC 0609.04, Initial

Characterization of Findings, and Exhibit 2 of IMC 0609, Appendix A, The Significance

Determination Process for Findings At-Power, issued June 19, 2012, the inspectors

screened the finding for safety significance and determined it to be of very low safety

significance (Green), since the finding did not represent an actual loss of system or

function. After inspector questioning, Entergy performed an operability evaluation, which

provided sufficient bases to conclude the Unit 3 baffle assembly would support ECCS

operability. This finding is related to the cross-cutting aspect of Problem Identification

and Resolution, Operating Experience, because Entergy did not effectively evaluate

relevant internal and external operating experience. Specifically, Entergy did not

adequately evaluate the impact of degraded baffle bolts at Unit 3 when relevant

operating experience was identified at Unit 2. [P.5]

Enforcement. 10 CFR 50, Appendix B, Criterion V, Instructions, Procedures, and

Drawings, states, in part, that activities affecting quality shall be prescribed by

documented procedures of a type appropriate to the circumstances and shall be

accomplished in accordance with those procedures. The introduction to Appendix B

states that quality assurance comprises all those planned and systematic actions

necessary to provide adequate confidence that a structure, system, or component (SSC)

will perform satisfactorily in service. Procedure EN-OP-104, Step 5.3[2], related to

immediate operability, states Determine if there is an ongoing degradation mechanism

that may impact future operability based on changing conditions, specifically consider

the SSCs specified safety function and mission time. Step 5.3(3) follows with, in part If

no Degraded or Non-conforming Condition exists, then perform the following as the

Immediate Determination: Declare the SSC Operable and Exit this procedure.

Contrary to the above, from May 5, 2016 until July 11, 2016, Entergy did not adequately

accomplish actions as prescribed by EN-OP-104 for a degraded condition associated

with the Unit 3 baffle-former bolts. Specifically, Entergy incorrectly concluded that no

18

degraded or non-conforming condition existed related to the Unit 3 baffle-former bolts

and exited the operability determination procedure. The NRC determined this is contrary

to EN-OP-104 because a comparison of Unit 2 and 3 operational factors resulted in

Entergy concluding that the Unit 3 baffle bolts would likely be affected due to the same

degradation mechanism. Entergys corrective actions included entering the issue into

the CAP and documenting an operability evaluation to support the basis for operability of

the baffle bolts and ECCS. Because this issue is of very low safety significance (Green)

and Entergy entered this into their CAP as CR-IP3-2016-01961, this finding is being

treated as an NCV consistent with Section 2.3.2.a of the Enforcement Policy. (NCV 05000286/2016002-02, Failure to Follow Operability Determination Procedure for

Unit 3 Baffle-Former Bolts)

Update to URI 05000247/2016001-06, 23 Emergency Diesel Generator Automatic

Voltage Regulator Failure

Introduction. The NRC opened a URI in Inspection Report 05000247/2016001 related to

two failures of the 23 EDG to run and maintain bus voltage on March 7, 2016, and to

provide adequate control of bus voltage on March 10, 2016. This report provides an

update of the status of this URI.

Description. On March 7, 2016, approximately one hour after the trip of the 3A normal

feed breaker, the 23 EDG tripped on overcurrent while powering the 6A 480V safety bus.

The 6A bus remained de-energized for approximately one hour until the crew restored

the 6A bus via off-site power. The 23 EDG was declared inoperable. All four 480V

safety buses were restored to off-site power. Entergy replaced the overcurrent relays

and retested the 23 EDG satisfactorily on March 8, 2016. However, bench testing of the

overcurrent relays demonstrated that they were accurately calibrated.

Subsequently, on March 10, 2016, during performance of PT-R14, Automatic Safety

Injection System Electrical Load and Blackout Test, the 23 EDG exhibited anomalous

behavior during the train B load sequencing. During this test, the voltage on safety bus

6A dropped to approximately 200V when the 23 auxiliary feedwater pump was

sequenced onto the bus (CR-IP2-2016-01430) and the sequencer failed to complete the

first two sequences. The 23 EDG was again declared inoperable and the period of

inoperability was backdated to March 7, 2016, when it originally tripped. Further

troubleshooting and additional failure modes analysis by Entergy initially determined that

the cause of both events may have been a degraded resistor (R25) on the 23 EDG

automatic voltage regulator (AVR) card.

The 23 EDG AVR card was replaced, and the 23 EDG was again tested satisfactorily.

The voltage anomaly issues exhibited during the March 10, 2016, test were documented

in CR-IP2-2016-01430 which was closed in CR-IP2-2016-01260 to be included in the

causal assessment associated with the tripping of 23 EDG breaker on March 7, 2016.

Entergy assigned a vendor to perform laboratory bench testing and failure analysis of

the 23 EDG AVR card. The vendor report attributed the cause of the March 10, 2016,

loss of voltage control to a degraded solder joint on the AVR card. However, the vendor

report explicitly did not attribute the event on March 7, 2016, to the same cause.

Entergy assigned a corrective action in CR-IP2-2016-01260 to review the cause of the

19

23 EDG overcurrent trip on March 7, 2016, in light of the vendor report. The inspectors

determined that the issue of concern remains open as a URI until this causal

assessment has been completed by Entergy and assessed by NRC. (URI

05000247/2016001-06, 23 Emergency Diesel Generator Automatic Voltage

Regulator Failure)

1R18 Plant Modifications (71111.18 - 2 samples)

Permanent Modifications

.1 Control Rod Guide Tube Repairs in Location E-9

a. Inspection Scope

The inspectors evaluated a modification to the reactor vessel upper internals to swap

damaged control rod guide tube in location E-9 with abandoned guide tube in location

D-10. The inspectors verified that the design bases, licensing bases, and performance

capability of the affected systems were not degraded by the modification. In addition,

the inspectors reviewed modification documents associated with the design change,

including evaluation of equivalency and core flow changes, and post-modification

testing. The inspectors also reviewed revisions to the affected drawings and interviewed

refueling and engineering personnel.

b. Findings

No findings were identified.

.2 Core Baffle-Former Bolt EC 64038

a. Inspection Scope

The inspectors reviewed EC 64038, IP2 Reactor Vessel Equivalent Replacement

Baffle-to-Former Bolt. This modification was completed during RFO 2R22 and involved

the replacement of 278 baffle-former bolts out of a total of 832 located in the Unit 2

reactor vessel. Entergy replaced all of the bolts that were potentially degraded as

observed by visual indications of a protruding bolt head or lock bar problem, bolts that

did not pass UT, and bolts inaccessible for UT. Entergy staff also replaced 51 additional

bolts that passed ultrasonic and visual examinations to increase the structural margin of

the baffle-former assembly for future operating cycles.

The inspectors reviewed the equivalency evaluation completed by Entergy staff to install

baffle-former bolts of a different material and configuration than the original bolts. The

inspectors reviewed the associated EC package to determine whether the replacement

bolts form, fit, and function were maintained compared to the original bolts and whether

the change conformed to the design and licensing bases of the baffle-former assembly.

Specifically, this change involved replacing the original baffle-former bolts made of

type 347 stainless steel with bolts made of type 316 stainless steel. The baffle-former

bolt head configuration was also changed from an original internal hex and slot design

(secured with a welded lock bar) to an external hex configuration with an integral locking

cup design. The design change document further evaluated a more gradual fillet

20

geometry between the bolt head and shank intended to reduce the stress concentration

at that transition and provide for improved fatigue resistance.

b. Findings

No findings were identified.

1R19 Post-Maintenance Testing (71111.19 - 8 samples)

a. Inspection Scope

The inspectors reviewed the post-maintenance tests for the maintenance activities listed

below to verify that procedures and test activities ensured system operability and

functional capability. The inspectors reviewed the test procedure to verify that the

procedure adequately tested the safety functions that may have been affected by the

maintenance activity, that the acceptance criteria in the procedure was consistent with

the information in the applicable licensing basis and/or design basis documents, and that

the test results were properly reviewed and accepted and problems were appropriately

documented. The inspectors also walked down the affected job site, observed the

pre-job brief and post-job critique where possible, confirmed work site cleanliness was

maintained, witnessed the test or reviewed test data to verify quality control hold points

were performed and checked, and that results adequately demonstrated restoration of

the affected safety functions.

Unit 2

21 EDG fuel oil transfer pump after planned maintenance on May 5, 2016

Replacement of pressurizer level transmitters LT-459 and LT-460 on May 25, 2016

21 CCW heat exchanger service water outlet weld repair on June 26, 2016

Flux mapping system drive repairs following motor failures on June 28, 2016

Unit 3

Maintenance on service water components associated with the 32 EDG on May 5,

2016 (this sample was part of an in-depth review of the EDG system)

Modification of the 32 EDG space heaters on May 5, 2016 (this sample was part of

an in-depth review of the EDG system)

Maintenance on the 32 EDG air start system on May 6, 2016 (this sample was part

of an in-depth review of the EDG system)

Replacement of failed bistable LC-427K, steam generator 32 low level mismatch trip

interlock, on May 18, 2016

b. Findings

No findings were identified.

21

1R20 Refueling and Other Outage Activities (71111.20 - 2 samples)

.1 Unit 2 RFO 2R22

a. Inspection Scope

The inspectors reviewed the stations work schedule and outage risk plan for the Unit 2

maintenance during RFO 2R22, which was conducted from March 7, 2016, to June 16,

2016. The inspectors reviewed Entergys development and implementation of outage

plans and schedules to verify that risk, industry experience, previous site-specific

problems, and defense-in-depth were considered. During the outage, the inspectors

observed portions of the shutdown and cooldown processes and monitored controls

associated with the following outage activities:

Configuration management, including maintenance of defense-in-depth,

commensurate with the outage plan for the key safety functions and compliance with

the applicable TSs when taking equipment OOS

Implementation of clearance activities and confirmation that tags were properly hung

and that equipment was appropriately configured to safely support the associated

work or testing

Installation and configuration of reactor coolant pressure, level, and temperature

instruments to provide accurate indication and instrument error accounting

Status and configuration of electrical systems and switchyard activities to ensure that

TSs were met

Monitoring of decay heat removal operations

Impact of outage work on the ability of the operators to operate the spent fuel pool

cooling system

Reactor water inventory controls, including flow paths, configurations, alternative

means for inventory additions, and controls to prevent inventory loss

Activities that could affect reactivity

Maintenance of secondary containment as required by TSs

Refueling activities, including fuel handling and fuel receipt inspections

Fatigue management

Tracking of startup prerequisites, walkdown of the primary containment to verify that

debris had not been left which could block the ECCS suction strainers, and startup

and ascension to full power operation

Foreign Object Search and Retrieval for missing baffle bolts and locking tabs

Identification and resolution of problems related to RFO activities

During this outage, Entergy replaced 278 degraded baffle bolts in the Unit 2 reactor

vessel baffle assembly. This emergent project resulted in the extension of the outage

schedule from 30 days to 102 days.

b. Findings

Introduction. The inspectors identified a Green NCV of TS 5.4.1 for Entergys failure to

implement procedure OAP-007, Containment Entry and Egress. Specifically, workers

transiting the inner and outer crane wall sections of containment on June 11, 2016, failed

to maintain at least one (of two) flow channeling gate closed to ensure availability of the

containment sumps to provide suction for the ECCS.

22

Description. On June 11, 2016, in mode 4, in preparation for reactor startup, Entergy

was performing maintenance in containment required prior to mode 3, such as reactor

coolant pump motor balancing and steam flow transmitter troubleshooting. These

activities required scaffolds to be temporarily erected for workers to safely perform

maintenance. While transiting from the inner to outer section of containment, the

inspectors noted that both flow channeling gates were maintained open simultaneously

as workers carried scaffold poles and hardware out of the area.

In the event of a postulated LOCA, Unit 2 relies on two sumps to provide a suction

source for the internal recirculation pumps and residual heat removal pumps,

respectively, after the injection phase of the accident. The sumps have cylindrical

screens with large surface area and small holes to filter small debris and maintain

adequate net positive suction head for the associated pumps. The reactor cavity sump

and large intervening barriers prevent large debris generated from the accident, such as

insulation, from reaching and blocking the recirculation and containment sump screens.

Entergy procedure OAP-007, Containment Entry and Egress, precaution and limitation

step 2.30.2, states, In mode 1, 2, 3, or 4, entry inside the crane wall shall use the

double gate entry point via gates 17 and 23. One gate shall remain shut and secured at

all times to maintain flow channeling and sump operability. Securing gates requires a

padlock or nut and bolt closure from the outside. This will require posting a gate monitor

to allow exit. The inspectors noted, while a gate monitor was posted, both gates were

maintained open during passage and not secured with a padlock or nut and bolt closure.

Upon questioning by the inspectors, Entergy immediately coached the gate monitor and

restored the gates to an acceptable position. Entergy generated CR-IP2-2016-04036 to

address this issue.

Analysis. The inspectors determined that Energys failure to maintain either gate 17 or

gate 23 closed during passage in accordance with OAP-007 was a performance

deficiency. The performance deficiency was more than minor because it is associated

with the configuration control (shutdown equipment lineup) attribute and adversely

affected the Mitigating Systems cornerstone objective to ensure the availability,

reliability, and capability of systems that respond to initiating events to prevent

undesirable consequences (i.e., core damage). The inspectors evaluated the finding in

accordance with IMC 0609, Appendix G, Attachment 1, Exhibit 3, and determined that a

detailed risk evaluation was necessary because the finding represented a loss of system

safety function. A detailed risk assessment was conducted conservatively assuming

complete failure of the recirculation and containment sumps due to the performance

deficiency. Given that Unit 2 was in mode 4, in plant operating state 1, with a late time

window, the at-power simplified plant analysis risk model for large-break LOCAs was

determined to best model the degrade condition and plant response. An exposure time

of one day was assumed. No credit was assumed for the decrease in energy that would

be anticipated in a release during a LOCA in mode 4, nor the corresponding reduction in

debris generation. This was also considered conservative. Utilizing Systems Analysis

Program for Hands-On Integrated Reliability Evaluation, version 8.13, with Indian Point

Unit 2 Simplified Plant Analysis Risk Model, version 8.19, for the assumed conditions,

the change in core damage frequency was determined to be 7E-9. Therefore, this issue

represents a Green finding.

23

This finding had a cross-cutting aspect in the area of Human Performance, Avoid

Complacency, because Entergy did not consider potential undesired consequences of

actions before performing work and implement appropriate error-reduction tools.

Specifically, the work crew did not understand the requirements and potential

consequences prior to commencing work and the gate monitor did not enforce these

requirements to maintain at least one gate locked or pinned closed as required by

OAP-007. [H.12]

Enforcement. Unit 2 TS 5.4.1.a requires that the procedures listed in Attachment A to

Regulatory Guide 1.33, Quality Assurance Program Requirements, Revision 2, be

established and implemented. Attachment A states that instructions should be prepared,

as appropriate, for access to containment and changing modes of operation of the

ECCS. Entergy procedure OAP-007, Containment Entry and Egress, Step 2.30.2,

states, In mode 1, 2, 3, or 4, entry inside the crane wall shall use the double gate entry

point via gates 17 and 23. One gate shall remain shut and secured at all times to

maintain flow channeling and sump operability. Securing gates requires a padlock or nut

and bolt closure from the outside. Contrary to the above, on June 11, 2016, Entergy did

not maintain one gate secured at all times with a padlock or nut and bolt closure.

Entergy entered this issue into the CAP as CR-IP2-2016-04036. Because this violation

was of very low safety significance (Green), and Entergy entered this performance

deficiency into the CAP, the NRC is treating this as a NCV in accordance with

Section 2.3.2.a of the NRC Enforcement Policy. (NCV 05000247/2016002-03, Failure

to Maintain Flow Channeling Gates Closed in Accordance with the Containment

Procedure)

.2 Unit 2 Forced Outage

a. Inspection Scope

Unit 2 conducted a forced outage from June 24 to 27, 2016, in order to complete weld

repairs on a through-wall leak on the service water inlet line to the 21 CCW heat

exchanger. These repairs required shutting down to mode 4 in order to meet the

TS 3.7.7, Component Cooling Water (CCW) System, limiting condition for operations

for CCW operability. While these repairs were being completed, the grid operator

completed repairs to breaker 9 in the offsite switchyard. During the outage, the

inspectors observed portions of the shutdown and cooldown processes and monitored

controls associated with the following outage activities:

Configuration management, including maintenance of defense-in-depth,

commensurate with the outage plan for the key safety functions and compliance with

the applicable TSs when taking equipment OOS

Implementation of clearance activities and confirmation that tags were properly hung

and that equipment was appropriately configured to safely support the associated

work or testing

Status and configuration of electrical systems and switchyard activities to ensure that

TSs were met

Monitoring of decay heat removal operations

Reactor water inventory controls, including flow paths, configurations, alternative

means for inventory additions, and controls to prevent inventory loss

Activities that could affect reactivity

24

Tracking of startup prerequisites

Identification and resolution of problems related to RFO activities

When all repairs had been completed, Entergy restarted Unit 2 on June 27, 2016.

b. Findings

No findings were identified.

1R22 Surveillance Testing (71111.22 - 6 samples)

a. Inspection Scope

The inspectors observed performance of surveillance tests and/or reviewed test data of

selected risk-significant SSCs to assess whether test results satisfied TSs, the UFSAR,

and Entergys procedure requirements. The inspectors verified that test acceptance

criteria were clear, tests demonstrated operational readiness and were consistent with

design documentation, test instrumentation had current calibrations and the range and

accuracy for the application, tests were performed as written, and applicable test

prerequisites were satisfied. Upon test completion, the inspectors considered whether

the test results supported that equipment was capable of performing the required safety

functions. The inspectors reviewed the following surveillance tests:

Unit 2

WO 446385, 21 EDG AVR card inspection, on May 24, 2016

2-PT-Q013 for containment isolation valve 851B (22 safety injection (SI) pump tie to

23 SI pump discharge) on June 6, 2016

2-PT-Q029B quarterly in-service surveillance test for the 22 SI pump on June 6,

2016

Unit 3

3-PT-M079B 32 EDG monthly surveillance on May 30, 2016 (this sample was part of

an in-depth review of the EDG system)

34 steam generator pressure instrument channel check on June 21, 2016

0-SOP-LEAKRATE-001, RCS Leakrate Surveillance, Evaluation and Leak

Identification, beginning on June 28, 2016

b. Findings

No findings were identified.

Cornerstone: Emergency Preparedness

25

1EP6 Drill Evaluation (71114.06 - 1 sample)

Training Observations

a. Inspection Scope

The inspectors evaluated the conduct of Entergys ingestion pathway emergency

preparedness drill on April 19, 2016, to identify any weaknesses and deficiencies in the

classification, notification, and protective action recommendation development activities.

The inspectors observed emergency response operations in the emergency operations

facility to determine whether the event classification, notifications, and protective action

recommendations were performed in accordance with procedures. The inspectors also

attended the facility drill critique to compare inspector observations with those identified

by Entergy staff in order to evaluate Entergys critique and to verify whether the staff was

properly identifying weaknesses and entering them into the CAP.

b. Findings

No findings were identified.

2. RADIATION SAFETY

Cornerstone: Public Radiation Safety and Occupational Radiation Safety

2RS1 Radiological Hazard Assessment and Exposure Controls (71124.01)

a. Inspection Scope

During May 10-12 and June 13-17, 2016, the inspectors reviewed Entergys

performance in assessing the radiological hazards and exposure control in the

workplace. The inspectors used the requirements in 10 CFR 20, TSs, applicable

industry standards, and procedures required by TSs as criteria for determining

compliance.

Radiological Hazards Control and Work Coverage

The inspectors reviewed:

Ambient radiological conditions during tours of the radiological controlled area,

posted surveys, radiation work permits, adequacy of radiological controls, radiation

protection job coverage, and contamination controls

Controls for highly activated or contaminated materials stored within spent fuel pools

Posting and physical controls for high radiation areas and very high radiation areas

b. Findings

No findings were identified.

26

2RS2 Occupational As Low As Is Reasonably Achievable (ALARA) Planning and Controls

(71124.02)

a. Inspection Scope

During May 10-12 and June 13-17, 2016, the inspectors assessed performance with

respect to maintaining occupational individual and collective radiation exposures ALARA.

The inspectors used the requirements in 10 CFR 20, TSs, applicable industry standards,

and procedures required by TSs as criteria for determining compliance.

Radiological Work Planning

The inspectors reviewed:

ALARA work activity evaluations, exposure estimates, and exposure mitigation

requirements

ALARA work planning, use of dose mitigation features and dose goals

Work planning and the integration of ALARA requirements

b. Findings

No findings were identified.

2RS7 Radiological Environmental Monitoring Program (REMP) (71124.07 - 3 samples)

a. Inspection Scope

The inspectors reviewed the REMP to validate the effectiveness of the radioactive

gaseous and liquid effluent release program and implementation of the groundwater

protection initiative (GPI). The inspectors used the requirements in 10 CFR 20,

40 CFR 190, 10 CFR 50, Appendix I, TSs, offsite dose calculation manual (ODCM),

Nuclear Energy Institute 07-07, and procedures required by TSs as criteria for

determining compliance.

Inspection Planning

The inspectors reviewed Entergys 2014 and 2015 annual radiological environmental

and effluent monitoring reports, REMP program audits, ODCM changes, land use

census, the UFSAR, and inter-laboratory comparison program results.

Site Inspection

The inspectors walked down various thermoluminescent dosimeter and air and water

sampling locations and reviewed associated calibration and maintenance records. The

inspectors observed the sampling of various environmental media as specified in the

ODCM and reviewed any anomalous environmental sampling events including

assessment of any positive radioactivity results. The inspectors reviewed any changes

to the ODCM. The inspectors verified the operability and calibration of the

meteorological tower instruments and meteorological data readouts. The inspectors

reviewed environmental sample laboratory analysis results, laboratory instrument

measurement detection sensitivities, laboratory quality control program audit results, and

27

the inter- and intra-laboratory comparison program results. The inspectors reviewed the

groundwater monitoring program as it applies to selected potential leaking SSCs.

GPI Implementation

The inspectors reviewed groundwater monitoring results, changes to the GPI program

since the last inspection, anomalous results or missed groundwater samples, leakage or

spill events including entries made into the decommissioning files (10 CFR 50.75(g)),

evaluations of surface water discharges, and Entergys evaluation of any positive

groundwater sample results including appropriate stakeholder notifications and effluent

reporting requirements.

Identification and Resolution of Problems

The inspectors evaluated whether problems associated with the REMP were identified at

an appropriate threshold and properly addressed in Entergys CAP.

b. Findings

No findings were identified.

4. OTHER ACTIVITIES

4OA1 Performance Indicator Verification (71151 - 6 samples)

Initiating Events Performance Indicators

a. Inspection Scope

The inspectors reviewed Entergys submittals for the following Initiating Events

cornerstone performance indicators for the period April 1, 2015, to March 31, 2016:

Unit 2

Unplanned scrams per 7000 critical hours (IE01)

Unplanned power changes per 7000 critical hours (IE03)

Unplanned scrams with complications (IE04)

Unit 3

Unplanned scrams (IE01)

Unplanned power changes (IE03)

Unplanned scrams with complications (IE04)

To determine the accuracy of the performance indicator data reported during those

periods, inspectors used definitions and guidance contained in Nuclear Energy

Institute 99-02, Regulatory Assessment Performance Indicator Guideline, Revision 7.

The inspectors reviewed Entergys operator narrative logs, maintenance planning

schedules, CRs, event reports, and NRC integrated inspection reports to validate the

28

accuracy of the submittals. There were no unplanned power changes or scrams with

complications during the review period.

b. Findings

No findings were identified.

4OA2 Problem Identification and Resolution (71152 - 4 samples)

.1 Routine Review of Problem Identification and Resolution Activities

a. Inspection Scope

As required by Inspection Procedure 71152, Problem Identification and Resolution, the

inspectors routinely reviewed issues during baseline inspection activities and plant

status reviews to verify that Entergy entered issues into the CAP at an appropriate

threshold, gave adequate attention to timely corrective actions, and identified and

addressed adverse trends. In order to assist with the identification of repetitive

equipment failures and specific human performance issues for follow up, the inspectors

performed a daily screening of items entered into the CAP and periodically attended CR

screening meetings. The inspectors also confirmed, on a sampling basis, that, as

applicable, for identified defects and non-conformances, Entergy performed an

evaluation in accordance with 10 CFR 21.

b. Findings

No findings were identified.

.2 Semi-Annual Trend Review

a. Inspection Scope

The inspectors performed a semi-annual review of site issues, as required by Inspection

Procedure 71152, Problem Identification and Resolution, to identify trends that might

indicate the existence of more significant safety issues. In this review, the inspectors

included repetitive or closely-related issues that may have been documented by Entergy

outside of the CAP, such as trend reports, performance indicators, major equipment

problem lists, system health reports, maintenance rule assessments, and maintenance

or CAP backlogs. The inspectors also reviewed Entergys CAP database for the first

and second quarters of 2016 to assess CRs written in various subject areas (equipment

problems, human performance issues, etc.), as well as individual issues identified during

the NRCs daily CR review (Section 4OA2.1). The inspectors reviewed the Entergy

quarterly trend report for the first quarter of 2016 to verify that Entergy was appropriately

evaluating and trending adverse conditions in accordance with applicable procedures.

b. Findings and Observations

No findings were identified.

The inspectors identified a trend in work being performed that was contrary to written

work instructions and procedures, and work packages had been closed out without

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documenting the deviation from the work order. While reviewing completed work order

WO 447966 Task 10, Internal Coating Repair for 21 CCW HX, the inspectors found a

note in the work order stating that the internal coating repair to the pipe had not been

done in accordance with the engineering change. The engineering change had been

written when the coating repair was expected to be small, but the actual area that was

recoated was much larger. A larger area of coating increases the impact on the heat

exchanger if the coating were to flake off and block the flow of service water. The work

package was closed and no condition report was written. This performance deficiency is

minor because the coating was applied with procedurally directed quality controls and

the likelihood that it would flake off is very small; and is the same as the original smaller

area specified in the work package. However, the work package was closed without

documenting the deviation and no CR was written.

In another example, the inspectors noted that WO 412920 Task 15 to perform a surge

test on 11 centrifugal air compressor (CENTAC) after overhaul was completed on

December 22, 2015. However, the completion notes and documentation for the task

showed that the test was unable to be performed due to a test equipment problem. The

work package was closed and no CR was written. Subsequently, after being returned to

service, the compressor failed in service due to multiple surging events on January 7,

2016. Troubleshooting under WO 433939 revealed that the motor high load limit had not

been adjusted to account for the increased load due to reduced compressor clearances

introduced by the overhaul. This performance deficiency is screened to minor because

the 11 CENTAC is not a safety-related piece of equipment and would not affect the MC 0609 cornerstone thresholds or other generic criteria. Unit 2 and Unit 3 have dedicated

instrument air compressors that are credited in the FSAR to respond to a loss of

instrument air event. If the 11 CENTAC (located in Unit 1) were to fail, the unit-specific

IACs would automatically start to prevent a loss of instrument air at both Units 2 and 3.

A third recent example of work being performed contrary to written instructions occurred

during 2RFO22 when the inspectors identified that the workers deviated from the

surveillance procedure by demonstrating the installation of the emergency containment

hatch plug without properly inflating the plug seals as directed by the procedure. This

performance deficiency was previously documented in a prior inspection report as non-

cited violation 05000247/05000286/2016001-02, Failure to Adequately Implement Risk

Management Actions for the Containment Key Safety Function.

In all cases, the deviations from written work instructions were directed by Entergy

supervision. In addition, the inspectors noted that Entergy had self-identified similar

observations where work packages or condition reports had been closed without fully

completing the specified actions including CR-IP2-2015-05833, CR-IP2-2016-00103,

CR-IP3-2015-04729, CR-IP3-2016-00072, CR-IP3-2016-00075, and CR-IP3-2015-

04019. These CRs are further examples of work orders that were closed with deviations

that were not documented or resolved. Nuclear Oversight had identified several of these

condition reports. Entergy has taking immediate corrective action in response to these

performance deficiencies.

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.3 Annual Sample: Maintenance Rule Self-Assessment of Corrective Actions

a. Inspection Scope

The inspectors performed an in-depth review of Entergys corrective actions associated

with self-assessment LO-IP3LO-2015-72, Maintenance Rule (a)(3) Assessment. The

self-assessment was performed to satisfy both the self-assessment criteria in EN-LI-104,

Self-Assessment and Benchmark Process, and the maintenance rule periodic

assessment criteria in EN-DC-207.

The inspectors assessed Entergys problem identification threshold, extent of condition

reviews, and the prioritization and timeliness of Entergy corrective actions to determine

whether Entergy was appropriately identifying, characterizing, and correcting problems

associated with this issue and whether the planned or completed corrective actions were

appropriate. The inspectors compared the actions taken to the requirements of

Entergys CAP and 10 CFR 50, Appendix B. In addition, the inspectors interviewed

engineering personnel to assess the effectiveness of the implemented corrective

actions.

b. Findings and Observations

No findings were identified.

Entergy identified three standard deficiencies during their self-assessment and wrote

CRs to document each one. One of the standard deficiencies was that the maintenance

rule basis documents were not being reviewed at least once every two years as required

by procedure EN-DC-204, Maintenance Rule Scope and Basis. The purpose of this

review was to ensure that the documents were updated if the configuration of the system

changed or if the performance criteria needed to be adjusted. Entergy wrote CR-IP3-

2015-03628 and assigned a corrective action to create work trackers to perform the

basis document reviews. They chose to use work trackers instead of corrective actions

under the CAP because the work had historically been assigned using work trackers.

However, because work trackers do not receive the same priority as corrective actions,

some of the maintenance rule basis documents had still not been reviewed at the time of

this inspection, over a year after the completion of the self-assessment. The inspectors

determined that this was not a more than minor issue because the systems in question

did not show signs of inadequate maintenance.

.4 Annual Sample: Unit 2 Reactor Trip on December 5, 2015

a. Inspection Scope

The inspectors performed an in-depth review of Entergys evaluations and corrective

actions associated with CR-IP2-2015-05484 and the related apparent cause evaluation

for the December 5, 2015, manual reactor trip in response to indications of multiple

dropped control rods caused by the loss of control rod power due to a power supply

failure. Entergy performed an apparent cause evaluation and determined the direct

cause of the event was the loss of motor control center (MCC)-24 due to an internal fault

at the line side leads at cubicle 2H where they connect to the bucket stab assemblies.

The apparent cause was an unanticipated loss of power to the control rod system due to

the degradation of the primary control rod power supply (PS1) which failed to function for

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more than 10 minutes when the operating alternate power supply (PS2) was

deenergized.

The inspectors assessed Entergys problem identification threshold, problem analysis,

extent of condition reviews, compensatory actions, and the prioritization and timeliness

of Entergy's corrective actions to determine whether Entergy was appropriately

identifying, characterizing, and correcting problems associated with this issue and

whether the planned or completed corrective actions were appropriate. The inspectors

compared the actions taken to the requirements of Entergy's CAP and 10 CFR 50,

Appendix B, Criterion XVI, Corrective Action.

b. Findings and Observations

No findings were identified.

The inspectors found that Entergy took appropriate actions to identify the direct and

apparent cause of the issue. The direct cause of the event was the loss of MCC-24 due

to an internal fault at the line side leads at cubicle 2H where they connect to the bucket

stab assemblies. The apparent cause was an unanticipated loss of power to the control

rod system due to the degradation of the primary control rod PS1, which failed to

function when PS2 was lost. Entergy replaced the degraded rod control PS1; and the

MCC-24 compartments were removed to facilitate inspection and testing of the MCC

bus, control wires, and MCC internal. PS2 was also restored to operation after the fault

was cleared.

The inspector determined that the internal electrical fault that deenergized PS2 and the

prior degradation in PS1 was not within Entergys ability to foresee and prevent.

Therefore, there was no performance deficiency identified. Entergys overall response to

the issue was commensurate with the safety significance, was timely, and the actions

taken and planned were reasonable to resolve the failure of the primary control rod PS1.

.5 Annual Sample: Unexpected Number of Degraded Baffle-Former Bolts Discovered in

the Unit 2 Reactor Pressure Vessel

a. Inspection Scope

The inspectors performed an in-depth review of Entergys root cause evaluation and

corrective actions associated with CR-IP2-2016-02348 for baffle-former (baffle) bolts

found with indications of degradation during the Indian Point Unit 2 RFO 2R22. Entergy

performed ultrasonic examinations of the baffle bolts in accordance with their procedures

as part of a planned activity. After an unexpected number of degraded baffle bolts were

discovered, Entergy staff reported the issue to the NRC as Event Notification 51829

on March 29, 2016, because the as-found number and location of degraded bolts

represented an unanalyzed condition. Entergy staff completed corrective actions to

replace all of the potentially degraded baffle bolts on Unit 2. Entergy staff further

replaced a population of additional bolts that exhibited no indications of degradation and

performed an evaluation to determine the potential for baffle bolt failures at Unit 3.

The baffle-former bolts help secure vertical plates (also referred to as baffle plates)

inside the reactor vessel, which then forms a structure surrounding the reactor fuel

assemblies to orient the fuel and to direct coolant flow through the core. A sufficient

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number of baffle bolts are required to remain intact to secure the baffle plates in place so

as to not affect control rod insertion or impede emergency core cooling flow during

postulated accident conditions. Bolt heads that separate and are no longer held in place

by bolt lock-tabs can also become a loose parts concern.

The inspectors determined whether Entergys acceptable baffle bolt pattern analysis for

Unit 2 was completed in accordance with the NRC-approved methodology and provided

appropriate structural margin for the next cycle of operation to ensure the Unit 2 baffle

plates will remain in place during both normal operation and limiting postulated accident

conditions. The inspectors further determined whether Entergys evaluations of the

baffle bolts installed in Indian Point Unit 3 were technically sufficient to conclude the

Unit 3 baffle assembly will perform as intended until the next planned RFO, at which time

Entergy plans to examine the bolts. The inspectors reviewed Entergys procedures for

determining the functionality and operability of degraded SSC as they relate to Unit 3.

The inspectors further interviewed Entergy engineering personnel and contractor staff to

discuss the results of Entergys technical evaluations and to assess the effectiveness of

the implemented and planned corrective actions.

The inspectors assessed Entergys problem identification threshold, cause analyses,

extent of condition, compensatory actions, and the prioritization and timeliness of

Entergys corrective actions to determine whether Entergy staff were properly identifying,

characterizing, and correcting problems associated with this issue and whether the

planned or completed corrective actions were appropriate. The inspectors compared the

actions taken to Entergys CAP, operability determination process, and the requirements

of 10 CFR 50, Appendix B. The inspectors observed portions of baffle bolt replacement

activities at Unit 2 and reviewed the final visual examination of the baffle bolts and plates

once the work was completed.

b. Findings and Observations

One Green NCV was identified and documented in Section 1R15 of this report.

The NRC responded to the initial discovery of an unexpected number of baffle bolts

found degraded at Indian Point Unit 2 by implementing a comprehensive inspection plan

consisting of various baseline inspection samples to assess the extent of the issue and

to determine the necessary NRC actions. A follow-up inservice inspection sample

(Refer to Section 1R08) was conducted to review the capability of the non-destructive

examination techniques, evaluate the UT results, and observe a portion of bolt

replacement activities on-site. A permanent modification sample (Refer to Section

1R18) was conducted to review the design change package and evaluations associated

with the new, replacement baffle bolts. The NRC resident inspectors reviewed Entergys

foreign material controls and loose parts analysis (Refer to Section 1R20) to address the

potential for missing bolt heads and concluded it would not impact safe operation of the

plant.

NRC Region I based inspectors accompanied by an expert from the NRC Office of

Nuclear Reactor Regulation completed an annual problem identification and resolution

inspection, documented in this section of the report, to verify that Entergys evaluations

and corrective actions to replace Unit 2 baffle bolts were completed in accordance with

an NRC approved methodology to support a conclusion that the Unit 2 baffle assembly

meets the plant design basis. The inspectors also determined the adequacy of

Entergys evaluations completed to determine there is a reasonable expectation that the

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Unit 3 baffle assembly will perform as intended during the current operating cycle. The

results of this review are discussed herein and in Section 1R15 of this report.

Entergy staff determined the cause of the degraded baffle bolts was primarily due to

IASCC in combination with increased fatigue loading on the baffle plates. This cause

determination was based on industry operating experience related to baffle-former bolt

failure in both foreign and domestic plants. IASCC is a cracking mechanism that occurs

over a long period of time when susceptible metals are exposed to neutron radiation

from the reactor core and stresses as part of normal design and operation. Entergy staff

concluded that failure of a critical number of bolts in a localized area subsequently

imposed increased loading on adjacent bolts, which propagated failures and generated

the moderate clustered pattern observed in the examination results. No other

contributing causes were identified.

The inspectors reviewed Entergys root cause evaluation and the supporting operating

experience related to baffle bolt failures at other plants. The inspectors determined that

there is documented evidence in the existing technical literature (including materials

testing of bolts from other plants) and operating experience to conclude that the likely

cause is IASCC; however, the inspectors found that Entergy staff did not define the

cause of the fatigue failure mechanism. The inspectors noted that Entergy staff sent a

sample of baffle bolts removed from the reactor pressure vessel to a metallurgical

laboratory for detailed failure analysis and materials property testing. Entergy indicated

their plans to use the results of the laboratory testing to confirm the likely root cause.

The inspectors concluded that Entergy staff conducted an appropriate review to identify

the likely causes of the degraded baffle bolts and noted that further test results will be

used to confirm these causes.

Following identification of the degraded baffle bolts on Unit 2, Entergys immediate

corrective action was to analyze the as-found condition and begin replacing bolts that

either had visual indications of bolt failure (protruding bolt head for example), did not

pass UT examination, or were not accessible for UT examination. The as-found number

and pattern of these bolts exceeded the acceptance criteria in the plants analysis that

was prepared in advance of the baffle bolt examinations; therefore, Entergy reported this

discovery to the NRC as an unanalyzed condition. Entergy staff completed corrective

actions to replace all of the 227 potentially degraded baffle bolts, plus an additional 51

bolts for increased structural integrity, for a total of 278 bolts. The inspectors noted the

51 additional bolts were installed in strategic locations to prevent clustering of potential

bolt failures during the next operating cycle.

The inspectors determined that Entergy staff performed an acceptable bolt pattern

analysis that evaluated the replacement bolt pattern for Unit 2 and modeled the potential

for future bolt failures. The inspectors found the results of the analysis accounted for a

conservative failure rate of bolts and provided appropriate margin for one cycle of

operation. The inspectors verified that Entergys methodology for its acceptable bolt

pattern analyses, including its determination of margin, was consistent with the NRC-

approved methodology in topical report WCAP-15029-NP-A (ML15222A882). The

inspectors determined that Entergy staff tracked corrective actions to re-examine the

Unit 2 baffle bolts during the next planned RFO. The inspectors noted the new baffle

bolts were made of a material with improved resistance to IASCC and included an

improved design to reduce the stresses at the head to shank transition, both of which

are enhancements compared to the original bolts.

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As part of an extent of condition assessment, Entergy entered CR-IP3-2016-01035 in its

CAP to evaluate the potential for degraded baffle bolts on Unit 3. Entergy operators

performed an IOD and concluded that the baffle assembly was operable. Entergy staff

performed a subsequent extent of condition review that concluded Unit 3 would

experience less baffle bolt degradation than Unit 2 based on several plant factors.

Entergy also conducted sensitivity analyses to show acceptable bounding conditions in

the event of bolt failures. The inspectors reviewed Entergys evaluations and noted that

Entergy staff concluded there was not a degraded condition at Unit 3. In consideration

of the guidance in their operability procedure and operating experience from Unit 2 and

other plants, the NRC issued an NCV in this report because Entergy did not perform an

operability evaluation for Unit 3 as a follow-up to the immediate determination for the

potential impact on supported systems controlled by the TS (Refer to Section 1R15).

As a corrective action, Entergy staff performed an operability evaluation and

demonstrated that the Unit 3 baffle former assembly remained operable. The inspectors

concluded that this supplemental evaluation provided appropriate technical justification

for the continued operation of Unit 3 until the next RFO in spring 2017, at which time

Entergy plans to examine the baffle bolts. Entergy also implemented a corrective action

as part of an enhancement to plant operations to monitor the RCS for any signs of fuel

leakage, which could be an indicator of baffle bolt failures.

The inspectors reviewed Westinghouse Nuclear Safety Advisory Letter NSAL-16-1,

which discussed the results of recent baffle-former bolt inspections and provided

Westinghouses recommendations on this issue. The letter described the plants as most

susceptible (i.e. Tier 1a) to this degradation as Westinghouse 4-loop reactors limited to

those with a down-flow configuration and using Type 347 stainless steel bolts. The

inspectors noted the recommendation was to complete UT volumetric examination of the

baffle bolts at the next scheduled RFO, and that Entergy had already planned this action

for Unit 3. Entergy also planned a long-term corrective action to convert Units 2 and 3

from a down-flow baffle configuration to an up-flow configuration, which would

significantly reduce the load on baffle-former bolts and provide for increased structural

margin of the baffle-former assembly. The inspectors determined Entergys overall

response to the issue was commensurate with the safety significance, was timely, and

included appropriate compensatory actions. The inspectors concluded that the actions

completed and planned were reasonable to address the ongoing aging management of

baffle bolts.

4OA3 Follow Up of Events and Notices of Enforcement Discretion (71153 - 5 samples)

.1 Plant Events

a. Inspection Scope

For the plant events listed below, the inspectors reviewed and/or observed plant

parameters, reviewed personnel performance, and evaluated performance of mitigating

systems. The inspectors communicated the plant events to appropriate regional

personnel, and compared the event details with criteria contained in IMC 0309, Reactive

Inspection Decision Basis for Reactors, for consideration of potential reactive inspection

activities. As applicable, the inspectors verified that Entergy made appropriate

emergency classification assessments and properly reported the event in accordance

with 10 CFR 50.72 and 50.73. The inspectors reviewed Entergys follow-up actions

35

related to the events to assure that Entergy implemented appropriate corrective actions

commensurate with their safety significance.

Unit 2

Turbine trip occurred while synchronizing Unit 2 to the grid on June 15, 2016

Shutdown required by TS for repairs to a leak on the 21 CCW heat exchanger

service water inlet on June 23, 2016

Unit 3

Rapid power reduction from 100 percent to 45 percent power in response to a loss of

both heater drain pumps on May 26, 2016

b. Findings

No findings were identified.

.2 (Closed) Licensee Event Report (LER) 05000247/2015-003-00: Manual Reactor Trip

Due to Indications of Multiple Dropped Control Rods Caused by Loss of Control Rod

Power Due to a Power Supply Failure

The inspectors reviewed Entergys actions and reportability criteria associated with LER 05000247/2015-003-00, which was submitted to the NRC on February 3, 2016. On

December 5, 2015, control room operators initiated a manual reactor trip after observing

indications consistent with multiple dropped control rods following an alarm for the trip of

MCC-24/24A. No control rod indication was available due to MCC-24 being faulted and

de-energized. The direct cause of the event was the loss of MCC-24 due to an internal

fault at the line sides leads at cubicle 2H where they connect to the bucket stab

assemblies. The apparent cause was an unanticipated loss of power to the control rod

system due to the degradation of the primary control rod PS1 which failed to function

when the operating PS2 was lost. The inspectors determined that both the unexpected

failure of PS2 and the internal fault in PS1 was not within Entergys ability to foresee and

prevent and was not a performance deficiency. The inspectors reviewed the LER, the

associated apparent cause evaluation analysis, and interviewed Entergy staff. This LER

is closed.

.3 (Closed) LER 05000247/2016-003-00: TS Prohibited Condition Due to an Inoperable 21

MBFP Discharge Valve for Greater Than the TS Allowed Outage Time

The inspectors reviewed Entergys actions and reportability criteria associated with LER 05000247/2016-003-00, which was submitted to the NRC on May 6, 2016. On March 7,

2016, during the shutdown to enter 2RFO22, the control switch for the 21 MBFP was

tripped from the control room but the MBFP discharge valve BFD-2-21 failed to fully

close as designed. The MBFP discharge valve was declared inoperable and TS 3.7.3

Condition C was entered. The MFD-2-21 isolation valve was then manually closed. The

direct cause of the failure to close the MBFP discharge valve BFD-2-21 was the motor

operated valves (MOVs) close torque switch contact finger out of position. The

apparent cause was that the MOV preventative maintenance procedure lacked the level

of detail and direction due to an unrecognized susceptibility associated with the

orientation of the close torque switch contact finger bracket opening and spreading of

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the U shape bracket. The downward arrangement made it easier for the torque switch

contact finger to move out with spreading of the U shaped contact holder. The

inspectors reviewed the LER, the associated apparent cause evaluation analysis, and

interviewed Entergy staff. This LER is closed.

Introduction. The inspectors identified a Green NCV of 10 CFR 50.65(b)(1) for Entergys

failure to include a function of a safety-related system within the scope of the

maintenance rule program. Specifically, Entergy failed to include the feedwater isolation

function performed by the MBFP discharge valves, MBFPs, and feedwater regulating

valves and feedwater isolation valves which are required to remain functional during and

following a design basis event to mitigate the consequences of an accident, within the

scope of the maintenance rule monitoring program.

Description. On March 7, 2016, during an RFO, the control switch for the 21 MBFP was

positioned to trip and the 21 MBFP tripped as designed, but the MBFP discharge valve

BFD-2-21 failed to fully close. Entergy declared MBFP discharge valve BFD-2-21

inoperable and entered TS 3.7.3 Condition C. After troubleshooting, Entergy determined

the MOV close torque switch contact finger was out of position within the contact holder.

The misalignment allowed the contact finger to move out of the proper position causing

the MOV BFD-2-21 to fail to close. This is the same failure mechanism which caused

MOV BFD-2-21 to fail to close in 2010 which is referenced in CR-IP2-2010-07013. On

December 5, 2015, the 21 MBFP failed to trip and required closure of the steam

admission valves to secure it. This failure occurred because of contaminated control oil

that prevented the solenoid valves from operating.

The inspectors reviewed Entergys maintenance rule basis documents and identified the

feedwater isolation function was not properly included in the maintenance rule

monitoring program as required by 10 CFR 50.65(b)(1). The basis document for the

feedwater system did identify the need to monitor the feedwater isolation function under

the maintenance rule and stated that it would be monitored as a part of the vapor

containment supersystem. However, the basis document for the vapor containment

supersystem does not include the feedwater isolation components within the system

boundaries. As a result, when component failures occurred which affected the

feedwater isolation function, they were not reviewed to determine if they were

maintenance rule functional failures; and Entergy was unable to identify that the

performance of the main feedwater isolation equipment was not effectively controlled

through preventative maintenance. Entergy entered this issue into the CAP as

CR-IP2-2016-03963 and initiated actions to include the MBFP discharge valves into the

maintenance rule program.

Analysis. The failure to appropriately scope the safety-related feedwater isolation

function within the maintenance rule program was a performance deficiency. This

finding is more than minor because it is associated with the SSC and barrier

performance attribute of the Barrier Integrity cornerstone and affected the cornerstone

objective to provide reasonable assurance that physical design barriers protect the

public from radionuclide releases caused by accidents or events. Specifically, the failure

to properly scope the feedwater isolation function prevented Entergy from identifying that

equipment reliability was no longer effectively controlled through preventative

maintenance. Additionally, this issue is similar to example 7.d described in IMC 0612,

Appendix EProperty "Inspection Manual Chapter" (as page type) with input value "NRC Inspection Manual 0612,</br></br>Appendix E" contains invalid characters or is incomplete and therefore can cause unexpected results during a query or annotation process., Examples of Minor Issues, dated August 11, 2009. In accordance with

IMC 0609.04, Initial Characterization of Findings, and Exhibit 2 of IMC 0609, Appendix

37

A, The Significance Determination Process for Findings At-Power, issued June 19,

2012, the inspectors determined that the finding was of very low safety significance

(Green) because the finding did not represent an actual open pathway in the physical

integrity of reactor containment, containment isolation system, and heat removal

components. There are redundant methods of feedwater isolation. They include

tripping the MBFPs and closing the MBFP discharge valves, closing the main feedwater

regulating valves and low flow bypass valves, and closing the main feedwater isolation

valves. On both December 5, 2015, and March 7, 2016, the main feedwater regulating

valves and isolation valves were functional; so there was no loss of the ability to isolate

feedwater to mitigate accident and transient conditions.

This finding does not have a cross-cutting aspect, since the failure to scope this

equipment into the maintenance rule program was not recognized when Entergy

combined the maintenance rule basis documents for Units 2 and 3 in 2012 and as a

result, is not indicative of current licensee performance.

Enforcement. 10 CFR 50.65(b)(1) requires, in part, that the holders of an operating

license shall include within the scope of the monitoring program, specified in

10 CFR 50.65(a)(1), SSCs that are relied upon to remain functional during and following

design basis events. Contrary to the above, since the combined maintenance rule

scoping for Units 2 and 3 in 2012, Entergy failed to include within the scope of the

monitoring program specified in 10 CFR 50.65(a)(1), the safety-related MBFP discharge

valves. These SSCs are relied upon during and after design basis events to mitigate the

consequences of a feedwater line break accident inside containment. Entergys

corrective action included entering this issue into the corrective action program.

Because the violation was of very low safety significance (Green) and Entergy entered

this issue into their CAP as CR-IP2-2016-03963, this violation is being treated as an

NCV, consistent with Section 2.3.2.a of the NRC Enforcement Policy.

(NCV 05000247/2016002-04, Failure to Scope Safety-Related Main Boiler Feedwater

Pump Discharge Valves into the Maintenance Rule Program)

4OA5 Other Activities

.1 Groundwater Contamination

a. Inspection Scope

On February 5, 2016, Entergy notified the NRC of a significant increase in groundwater

tritium levels measured at three monitoring wells (MWs) (MW-30, MW-31, and MW-32)

located near the Unit 2 fuel storage building. These samples were drawn on

January 26 to 27, 2016, and analyzed and confirmed on February 2 to 4, 2016. The

highest concentration was detected at MW-32, which increased from 12,000 pCi/l on

January 11, 2016, to 8,100,000 pCi/l on January 26, 2016, and subsequently up to

14,800,000 pCi/l on February 4, 2016. This increased tritium concentration event was

documented by Entergy in CR-IP2-2016-00564 which documents its investigation of this

event including a root cause evaluation. The inspectors reviewed Entergys root cause

evaluation for this event during this inspection period as well as recent groundwater

monitoring results.

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b. Findings and Observations

No findings were identified.

Update to URI 05000247/2016001-07, January 2016 Groundwater Contamination

Entergy continues to conduct weekly, biweekly, and monthly groundwater sampling of

MWs at the initial site of groundwater contamination and at downstream wells towards

the Hudson River. For the initial three MWs (MW-30, MW-31, and MW-32), the general

trend in tritium activity has been downward, with periodic increases seen in some weekly

samples. The downstream MWs located in the Unit 2 switchyard (especially MW-55)

showed an initial increase in activity up to 117,000 pCi/l, but the activity at that location

has plateaued at the end of the reporting period.

Entergy documented its investigation of this event as root cause evaluation for

CR-IP2-2016-00564. The inspectors reviewed Entergys root cause evaluation for this

event. Entergy concluded that the source of the groundwater contamination was from

the reject water of a temporary reverse osmosis unit used to process water from the

refueling water storage tank at Unit 2 in preparation for RFO 2R22. Although this

analysis documents a number of issues identified during the operation of the contractor

reverse osmosis unit, which is believed to be the source of the groundwater

contamination, one of two leakage paths to groundwater have still not been established.

The established pathway involves leakage from two cut drain lines located above the

floor on the 35-foot elevation of the PAB. Further investigation by Entergy following the

conclusion of the Unit 2 RFO 2R22 must be conducted to verify the second pathway to

groundwater via the floor of the fuel storage building truck bay.

Entergys long-term corrective action for reducing tritium levels in the groundwater is the

same as previously identified for the March 2014 tritium spike (CR-IP2-2015-03806), the

start-up and operation of recovery well (RW)-1. Following installation of equipment and

system testing, full operation of the RW system is expected later this year. This system

will allow for the collection of tritiated groundwater in the vicinity of Unit 2 to be returned

inside the Unit 2 PAB for processing. The NRC will be conducting an inspection in

August 2016 to review the testing plan and results of the RW-1 tests. This inspection

will include a specialist region-based inspector, and a staff hydrogeologist.

The NRCs continuing assessment of the safety significance of this event focused on

validating the safety impact of dose to the public from the release of tritium to the site

groundwater, and ultimately to the Hudson River. The NRC verified that Entergys

bounding public dose calculations on the groundwater contamination leak was

sufficiently conservative and a maximum worst case scenario would result in a dose of

0.000112 millirem per year, which represents a very small fraction of the allowable dose

(liquid effluent dose objective of 3 millirem per year). This low value is due to

groundwater at Indian Point not being a source of any drinking water. There are no

drinking water wells on the Indian Point site, groundwater flow from the site is to the

Hudson River and not to any near site drinking water wells, and the Hudson River has

no downstream drinking water intakes as it is brackish water. Pathways to the public are

therefore limited to the consumption of fish and river invertebrates. The inspection

determined that there is no safety impact to the public as a result of this groundwater

contamination event. (URI 05000247/2016001-07, January 2016 Groundwater

Contamination)

39

.2 Institute of Nuclear Power Operations (INPO) Report Review

a. Inspection Scope

The inspectors also reviewed the final report for the INPO equipment reliability scram

review visit that was conducted to review the scrams that occurred over the past two

years, conducted in June 2016. The inspectors reviewed the report to ensure that any

issues identified were consistent with NRC perspectives of Entergy performance and to

determine if INPO identified any significant safety issues that required further NRC

follow-up.

b. Findings

No findings were identified.

4OA6 Meetings, Including Exit

On August 4, 2016, the inspectors presented the inspection results to Mr. Larry Coyle,

Site Vice President, and other members of Entergy. Based on additional information

provided, the inspectors conducted an updated exit meeting on August 30, 2016 with

John Kirkpatrick, Plant Operations General Manager and other members of Entergy.

The inspectors verified that no proprietary information was retained by the inspectors or

documented in this report.

ATTACHMENT: SUPPLEMENTARY INFORMATION

A-1

SUPPLEMENTARY INFORMATION

KEY POINTS OF CONTACT

Entergy Personnel

A. Vitale, Site Vice President

J. Kirkpatrick, Plant Operations General Manager

R. Alexander, Unit 2 Shift Manager

R. Andersen, Maintenance Instrumentation and Controls Superintendent

N. Azevedo, Engineering Supervisor

J. Baker, Shift Manager

S. Bianco, Operations Fire Marshal

K. Brooks, Assistant Operations Manager

R. Burroni, Engineering Director

T. Chan, Engineering Supervisor

C. Chapin, Training Superintendent

D. Dewey, Assistant Operations Manager

J. Dignam, Unit 3 Control Room Supervisor

R. Dolansky, Inservice Inspection Program Manager

W. Durr, Outage Control Center Manager

R. Drake, Engineering Supervisor

K. Elliott, Fire Protection Engineer

J. Ferrick, Regulatory and Performance Improvement Director

L. Frink, Radiation Protection Supervisor

D. Gagnon, Security Manager

L. Glander, Emergency Preparedness Manager

D. Gray, Radiological Environmental Manager

J. Johnson, Unit 2 Control Room Supervisor

M. Johnson, Unit 3 Shift Manager

M. Khadabux, Instrumentation and Controls Supervisor

F. Kich, Performance Improvement Manager

M. Lewis, Unit 3 Assistant Operations Manager

N. Lizzo, Training Manager

S. McAllister, Baffle Bolt Replacement Project Manager

M. McCarthy, Unit 3 Control Room Supervisor

B. McCarthy, Operations Manager

F. Mitchell, Radiation Protection Manager

E. Mullek, Maintenance Manager

S. Stevens, Radiation Protection Operations Superintendent

B. Sullivan, Training Superintendent

J. Taylor, Unit 3 Shift Manager

M. Tesoriero, Outage Control Center Manager

M. Troy, Nuclear Oversight Manager

R. Walpole, Regulatory Assurance Manager

A. Zastrow, Assistant Operations Manager

Attachment

A-2

LIST OF ITEMS OPENED, CLOSED, DISCUSSED, AND UPDATED

Opened

05000247/2016002-01 URI CVCS Goal Monitoring Under the Maintenance

Rule (Section 1R12)

Opened/Closed

05000286/2016002-02 NCV Failure to Follow Operability Determination

Procedure for Unit 3 Baffle-Former Bolts

(Section 1R15)05000247/2016002-03 NCV Failure to Maintain Flow Channeling Gates Closed

in Accordance with the Containment Procedure

(Section 1R20)05000247/2016002-04 NCV Failure to Scope Safety-Related Main Boiler

Feedwater Pump Discharge Valves into the

Maintenance Rule Program (Section 4OA3)

Closed

05000247/2015-003-00 LER Manual Reactor Trip due to Indications of Multiple

Dropped Control Rods Caused by Loss of Control

Rod Power Due to a Power Supply Failure

(Section 4OA3)

05000247/2016-003-00 LER Technical Specification Prohibited Condition

Due to an Inoperable 21 Main Boiler Feedwater

Pump Discharge Valve for Greater Than the TS

Allowed Outage Time (Section 4OA3)

Discussed

05000247/2016001-01 URI Baffle-Former Bolts with Identified Anomalies

(Section 1R08)05000247/2016001-06 URI Emergency Diesel Generator Automatic Voltage

Regulator Failure (Section 1R15)05000247/2016001-07 URI January 2016 Groundwater Contamination

Section (Section 4OA5)

A-3

LIST OF DOCUMENTS REVIEWED

Common Documents Used

Indian Point Unit 2 and Unit 3, UFSARs

Indian Point Unit 2 and Unit 3, Individual Plant Examinations

Indian Point Unit 2 and Unit 3, Individual Plant Examination of External Events

Indian Point Unit 2 and Unit 3, TSs and Bases

Indian Point Unit 2 and Unit 3, Technical Requirements Manuals

Indian Point Unit 2 and Unit 3, Control Room Narrative Logs

Indian Point Unit 2 and Unit 3, Plans of the Day

Section 1R04: Equipment Alignment

Procedures

2-COL-4.2.1, Residual Heat Removal System, Revision 30

2-COL-4.3.1, Spent Fuel Pit Cooling, Revision 10

2-COL-24.1.1, Service Water System, Revision 50

3-COL-EL-005, Diesel Generators, Revision 37

OAP-019, Component Verification and System Status Control, Revision 7

OAP-044, Plant Labeling Program, Revision 3

Condition Reports (CR-IP2)

2016-01311 2016-01505 2016-01761 2016-02330 2016-02428 2016-02470

Condition Reports (CR-IP3)

2016-01382 2016-01810

Drawings

209762, Flow Diagram Service Water System Nuclear Steam Supply Plant, Revision 75

227781, Flow Diagram Auxiliary Coolant System, Revision 22

9321-2720, Auxiliary Coolant System, Sheet 2, Revision 22

Miscellaneous

IP3-DBD-308, CCW System, Revision 3

Section 1R05: Fire Protection

Procedures

EN-MA-133, Control of Scaffolding, Revision 12

Condition Reports (CR-IP2)

2016-04148

Condition Reports (CR-IP3)

2016-01272

Miscellaneous

PFP-203, Containment Building, 95-Foot Elevation (Fire Zone 86A), Revision 15

PFP-204, General Floor Plan, PAB, 15-Foot Elevation, Revision 0

PFP-209, Component Cooling Pump Room, PAB, 68-Foot Elevation, Revision 0

PFP-211, General Floor Plan, PAB, 80-Foot Elevation, Revision 14

PFP-351, 480V Switchgear Room, Revision 15

A-4

Section 1R07: Heat Sink Performance

Procedures

0-HTX-405-EDG, EDG Lube Oil and Jacket Water Heat Exchanger Maintenance, Revision 4

Condition Reports (CR-IP3)

2010-02900 2011-03594 2011-03596 2011-03961 2012-02071 2012-03912

2013-02338 2013-02695 2013-03009 2014-00957 2014-01239 2014-03158

2014-03175 2015-00031 2015-00599 2015-02848 2015-05209 2015-05526

2016-00886 2016-00895 2016-00899

Maintenance Orders/Work Orders

WO 52489888 WO 52626563

Miscellaneous

SEP-SW-IPC-001, Indian Point Energy Center NRC Generic Letter 89-13 Service Water

Program, Revision 0

Section 1R08: Inservice Inspection Activities

Procedures

GBRA-104-659, Collection of Protocols for Baffle Bolt Replacement, Revision C

GBRA-175-115, Field Service Procedure for Baffle Bolt Replacement, Revision 3

WDI-STD-088, Underwater Remote Visual Examination of Reactor Vessel Internals,

Revision 13

WDI-STD-1073, Ultrasonic Test Procedure for the Inspection of Internal Hex Head

Baffle-Former Bolts with Welded Lock Bars, Revision 4

Condition Reports (CR-IP2)

2016-02081

Maintenance Orders/Work Orders

442412-13

Miscellaneous

Indian Point Unit 2 Baffle Bolt Ultrasonic Examination Expanded Analysis Report, dated

April 28, 2016

IP2 Reactor Vessel Visual Examination Report, dated May 2006

Loose Parts Inventory Log for Baffle Bolt Replacements, dated May 24, 2016

MRP-227-A, Materials Reliability Program: Pressurized Water Reactor Internals Inspection and

Evaluation Guidelines (ML120170453)

MRP-228, Materials Reliability Program: Inspection Standard for PWR Internals - 2012 Update,

Revision 1

SEP-ISI-IP2-001, IP2 Fourth Ten-Year Interval Inservice Inspection (ISI)/Containment Inservice

Inspection (CISI) Program Plan, Revision 2

WDI-PJF-1315504-EPP-001, Indian Point Nuclear Power Plant MRP-227-A Reactor Vessel

Internals Examination Program Plan, Revision 0

WDI-PJF-1315505-FSR-001, Indian Point Unit 2 2R22 MRP-227-A Baffle-Former Bolt

Ultrasonic Inspections Field Service Report, dated March 29, 2016

WDI-TJ-1100, Technical Justification for the Ultrasonic Inspection of Baffle-Former Bolts for

Indian Point Units 2 and 3, Revision 1

A-5

Section 1R11: Licensed Operator Requalification Program

Procedures

2-AOP-480V-1, Loss of Normal Power to Any 480V Vital Bus, Revision 8

2-AOP-RCP-1, Reactor Coolant Pump Malfunction, Revision 14

2-AOP-TURB-1, Main Turbine Trip without a Reactor Trip, Revision 5

2-E-0, Reactor Trip or Safety Injection, Revision 7

2-FR-H.1, Response to Loss of Secondary Heat Sink, Revision 11

2-POP-1.2, Reactor Startup, Revision 59

2-SOP-26.4, Turbine Generator Startup, Synchronizing, Voltage Control and Shutdown,

Revision 62

3-AOP-480V-1, Loss of Normal Power to Any Safeguards Bus, Revision 7

3-AOP-CVCS-1, Chemical and Volume Control System Malfunction, Revision 8

3-AOP-FW-1, Loss of Feedwater, Revision 8

3-AOP-INST-1, Instrument/Controller Failures, Revision 11

3-E-0, Reactor Trip or Safety Injection, Revision 6

3-E-1, Loss of Reactor or Secondary Coolant, Revision 4

3-FR-C.2, Response to Degraded Core Cooling, Revision 3

Condition Reports (CR-IP2)

2016-03946 2016-04162 2016-04164 2016-04165 2016-04169 2016-04178

Condition Reports (CR-IP3)

2016-01087 2016-01092 2016-01098 2016-01336

Miscellaneous

13SX-LOR-SES026, Licensed Operator Requalification Program Scenario

Emergency Action Level Table, Revision 15.2

LRQ-SES-04, IPEC Simulator Evaluated Scenario, Revision 6

Section 1R12: Maintenance Effectiveness

Procedures

CEP-NDE-0640, Non-Section XI Liquid Penetrant Examination, Revision 9

CEP-WP-WIIR-1, Attachment 5.1, Inprocess Inspections for Installation and Replacement

Welds Located Inside the ASME Section XI Boundary, Revision 3

EN-DC-206, Maintenance Rule (a)(1) Process, Revision 3

Condition Reports (CR-IP2)

2010-00864 2013-03130 2014-00162 2014-00185 2014-01144 2014-02184

2015-00278 2016-01260 2016-01430 2016-01500

Condition Reports (CR-IP3)

2012-03836 2013-04758 2015-01396 2015-03404 2015-03653 2015-04053

2015-04162 2015-04184 2015-04539 2015-05316 2015-05384 2015-05729

A-6

2016-00098 2016-00653 2016-00723 2016-01189 2016-01227 2016-01274

2016-01313 2016-01531 2016-01536 2016-01543 2016-02432

Maintenance Orders/Work Orders

WO 00397793 WO 00408019 WO 00414886 WO 00416091

WO 00421841 WO 00429532 WO 00429532 WO 00431497

WO 00446165 WO 00447042 WO 00447966 WO 52602429

WO 52621178

Miscellaneous

EC 65389, 21 CCW HX Leak Repair: Service Water Inlet Nozzle - Elbow Weld Configuration

Change

IPEC Maintenance Rule Basis Document - Chemical and Volume Control System, Revision 0

PQR 913, 134 F42 MN-GTAW ASME IX Welding Procedure Qualification Record, Revision 0

System Health Report, Unit 3, EDG, Q1-2016

Weld Map Number 447966-20-01, Revision 0

WPS 134 F42, MN-GTAW, ASME Section IX Welding Procedure Specification, Revision 0

Section 1R13: Maintenance Risk Assessments and Emergent Work Control

Procedures

EN-OP-119, Protected Equipment, Revision 8

IP-SMM-OU-104, Attachment 9.1, Shiftly Outage Shutdown Safety Assessments, Revision 15

IP-SMM-OU-104, Attachment 9.2, Shiftly Outage Shutdown Safety Assessment Guidelines,

Revision 15

Condition Reports (CR-IP2)

2016-04141

Condition Reports (CR-IP3)

2016-01545

Miscellaneous

EOOS Risk Assessment Software Tool

Section 1R15: Operability Determinations and Functionality Assessments

Procedures

2-PC-R3-1, Pressurizer Level Transmitters, Revision 10

3-ARP-010, Metal Impact Monitoring System, Page 10, Revision 32

3-SOP-RCS-016, Operation of the Metal Impact Monitoring System, Revision 8

EN-OP-104, Operability Determination Process, Revision 10

Condition Reports (CR-IP2)

2016-2221 2016-2356 2016-2961 2016-3345 2016-3418 2016-3660

2016-3636 2016-3784 2016-3806 2016-3818 2016-4085

Condition Reports (CR-IP3)

2014-01670 2015-03468

A-7

Maintenance Orders/Work Orders

WO 00327574 WO 00425980 WO 52571030

Miscellaneous

EN-LI-100, Attachment 9.1, Change Channel Check Comparison Criteria/2-PT-M100,

2-PT-D001, Revision 0

Section 1R18: Plant Modifications

Drawings

10073E87-001, Indian Point Unit 2 Baffle Bolt Replacement - Core Barrel and Baffle Assembly

Elevation, Revision 0

10111D06, Indian Point Unit 2 Baffle Bolt Replacement - Replacement Baffle Bolt .625

and .750, Revision 0

Miscellaneous

EC 64308, IP2 Reactor Vessel Equivalent Replacement Baffle-to-Former Bolt, Revision 0

Process Applicability Determination Form for EC 64308, dated April 21, 2016

WCAP-18136-P, Replacement Type 316 Cold-Worked Baffle-Former Bolt Qualification for

Indian Point Unit 2, Revision 0

Section 1R19: Post-Maintenance Testing

Procedures

3-PT-M079B, 32 EDG Functional Test, Revision 52

2-PC-Q109-4, Recalibration of NIS and OT/OP Delta-T Parameters - Channel IV, Revision 44

Condition Reports (CR-IP2)

2016-03961 2016-04266

Condition Reports (CR-IP3)

2016-01189 2016-01199 2016-01218

Maintenance Orders/Work Orders

WO 00414886 WO 00420649 WO 00446094 WO 00447966

WO 52545181 WO 52626563 WO 52626564 WO 52630619

WO 52630620 WO 52658943 WO 00236158 WO 00277374

WO 52571030

Drawings

5651D72, Logic Diagrams Steam Generator Trip Signals, Revision 7

Miscellaneous

EC 64545, Emergency Temporary Modification to Disconnect 32 EDG Generator Space Heater

Adjacent to End Plate on Outboard End of Generator

FIX00091, Pressurizer Level Uncertainty - Indication, Trip Setpoints, and Annunciation

Setpoints, Revision 1

E-mail from J. Michetti to G. Newman, dated July 19, 2016, Subject: Westinghouse Report

on E9

A-8

Section 1R20: Refueling and Other Outage Activities

Procedures

2-POP-1.1, Plant Heatup from Cold Shutdown, Revision 90

2-POP-1.2, Reactor Startup, Revision 59

2-POP-1.3, Plant Startup from Zero to 45 Percent Power, Revision 89

2-POP-3.1, Plant Shutdown from 45 Percent Power, Revision 58

2-POP-3.3, Plant Cooldown, Hot to Cold Shutdown, Revision 81

2-POP-3.4, Secondary Plant Shutdown, Revision 10

2-POP-4.1, Operation at Cold Shutdown, Revision 5

2-POP-4.2, Operation Below 20 Percent Pressurizer Level with Fuel in the Reactor, Revision 8

2-POP-4.3, Operation without Fuel in the Reactor, Revision 1

Condition Reports (CR-IP2-)

2016-04118 2016-04119 2016-04123 2016-03124 2016-04126 2016-04129

2016-04130 2016-04131 2016-04132 2016-04139 2016-04141* 2016-04142*

2016-04144 2016-04145 2016-04146 2016-04148* 2016-04151 2016-04152

2016-04155 2016-04161 2016-04162 2016-04165 2016-04169

  • NRC identified

Maintenance Orders/Work Orders

52681465

Miscellaneous

2R22 Performance Indicator Curves Daily from March 7 to June 14, 2016

Outage Schedules and Plans of the Day from March 7 to June 14, 2016

Westinghouse LTR-PL-16-16, Operability Assessment for Primary Side Loose Parts at Indian

Point Unit 2, Revision 0, dated March 27, 2016

Section 1R22: Surveillance Testing

Procedures

0-SOP-LEAKRATE-001, RCS Leakrate Surveillance Evaluation and Leak Identification,

Revision 6

2-PT-D001, Control Room Operations Surveillance Requirements, Revision 16

2-PT-M029B, 22 Safety Injection Pump, Revision 20

2-PT-Q013, Inservice Valve Tests, Revision 51

2-PT-Q013-DS040, Valve 887B Inservice Test Data Sheet, Revision 22

3-PT-M079B, 32 EDG Functional Test, Revision 52

Condition Reports (CR-IP2)

2016-03360 2016-03363

Condition Reports (CR-IP3)

2016-01716 2016-01752

Maintenance Orders/Work Orders

WO 00443040 WO 00446385 WO 00446867 WO 52681652-01

WO 52681646-01

A-9

Miscellaneous

EC 64855, EC Reply to Provide Input Regarding MPR Maintenance Bulletin MB-2007-01 for

Auto Voltage Regulator Solder Joints

MB-2007-01, Potential for Solder Joint Cracks on Basler SBSR Auto Voltage Regulator Cards

and Technical Manual Addendum TM-2007-01, November 5, 2007

Unit 3 RCS Routine Activity Sample, 28-June-16-10006

Section 1EP6: Drill Evaluation

Procedures

IP-EP-120, Emergency Classification, Revision 10

IP-EP-410, Protective Action Recommendations, Revision 11

Section 2RS7: Radiological Environmental Monitoring Program

Procedures

0-CY-1920, REMP Land Use Census, Revision 1

0-CY-1980, Preparation, Placement and Collection of Site Environmental Thermoluminescent

Dosimeters, Revision 2

Condition Reports (CR-IP2)

2014-05319 2015-00948 2015-01300 2015-02687 2015-02800 2015-02987

2015-03271 2015-03396 2016-02313

Condition Reports (CR-IP3)

2016-00514

Miscellaneous

2014 Annual Radiological Environmental Operating Report, Indian Point Nos. 1, 2, and 3

2015 Annual Radiological Environmental Operating Report, Indian Point Nos. 1, 2, and 3

Environmental Dosimetry Company, Annual Quality Assurance Status Report,

January to December 2015

Indian Point Energy Center ODCM, Revision 4

June 2015 to May 2016 Meteorological Data Recovery

Met One Instruments, Inc. Certificates of Calibration for Temperature, Wind Direction, and Wind

Speed

Teledyne Brown Engineering Environmental Services Annual 2015 Quality Assurance Report

Exelon PowerLabs Certificates of Calibration for Gas Meters

3471875 3482909 3471871 3471867 3482920 3471873

3482910 3482916 3471877 3482914 3482918 3482921

3471881 3471879 3471872 3471869 3471880 3482908

Quality Assurance

Quality Assurance Audit Report QA-2-6-2015-IP-1, Chemistry, Effluents, and Environmental

Monitoring Snapshot Self-Assessment, LO-IP3LO-2015-00126, Chemistry-REMP

Section 4OA2: Problem Identification and Resolution

Procedures

EN-DC-204, Maintenance Rule Scope and Basis, Revision 3

EN-DC-204, Maintenance Rule Scope and Basis, Revision 3

EN-DC-207, Maintenance Rule Periodic Assessment, Revision 3

A-10

EN-LI-102, Corrective Action Program, Revision 26

EN-LI-104, Self-Assessment and Benchmark Process, Revision 11

EN-LI-110-01, Equipment Failure Evaluation, Revision 0

EN-LI-119, Apparent Cause Evaluation Process, Revision 11

EN-OP-104, Operability Determination Process, Revision 10

Condition Reports (CR-IP2)

2010-07013 2015-04574 2015-05458 2015-05460 2015-05461 2015-05464

2015-05466 2015-05467 2016-01374 2016-02348

Condition Reports (CR-IP3)

2015-3628 2016-01035 2016-01961

Maintenance Orders/Work Orders

WO 00442412

Apparent Cause Evaluations

IP2-2015-05458

Drawings

504405, Sheet 1 of 2, Replacement Baffle Bolt Location Matrix, Revision 0

504405, Sheet 2 of 2, Replacement Baffle Bolt Location Matrix, Revision 0

Miscellaneous

61265, Temporary Modification Control Form-Install Additional Temporary Spare Power Supply

Inside Rod Control Cabinet 2BD to Restore Margin, Revision 0

Appendix A to Facility Operating License DPR-64, Technical Specifications and Basis For The

Indian Point 3 Nuclear Generating Station Unit No.3, Through Amendment 260

CN-RIDA-15-43, Indian Point Units 2 and 3 Acceptable Baffle-Former Bolting LOCA and

Seismic Analysis, Revision 2

Engineering Change 63938, As-left condition of the baffle-former plate assembly following the

replacement of degraded bolts, Revision 0

EPRI TR-112209, Analysis of Baffle Former Bolt Cracking in EDF CPO Plants (PWRMRP-03),

dated June 1999

Indian Point Entergy Center (IPEC) Unit 3, Updated Final Safety Analysis Report, dated May

2013

IP-RPT-16-00025, Evaluation of Indian Point Unit 3 Reactor Core Baffle Bolting Following MRP-

227-A Inspection Findings at Indian Point Unit 2 during 2R22, Revision 0

LO-IP3LO-2015-72

LTR-PL-16-21, Transmittal of Indian Point Unit 3 Final Engineering Evaluations Supporting

Extent of Condition Review, Revision 0

LTR-RIDA-16-103, Indian Point Unit 2 Baffle Bolting Anti-Clustering Pattern and Margin

Assessment, Revision 0

LTR-RIDA-16-152, Indian Point Unit 3 Baffle Bolt Leak Before Break Operability Assessment,

Revision 0

LTR-RIDA-16-60, Indian Point Unit 2 Baffle Bolting One Cycle Replacement Pattern Summary

Letter, Revision 0

MRP-227-A, Materials Reliability Program: Pressurized Water Reactor Internals Inspection and

Evaluation Guidelines (ML120170453)

Operation Decision Making Issue Action Plan for IP3 Baffle Bolt Monitoring, dated May 19, 2016

WCAP-15029-NP-A, Westinghouse Methodology for Evaluating the Acceptability of Baffle-

Former-Barrel Bolting Distributions Under Faulted Load Conditions, Revision 0

(ML15222A882)

A-11

WCAP-17949-P, Background and Technical Basis Supporting Engineering Flaw Acceptance

Criteria for Indian Point Unit 2 Reactor Vessel Internals MRP-227-A Primary and

Expansion Components, Revision 1

WCAP-18048-P, Determination of Acceptable Baffle-Former Bolting for Indian Point Units 2 and

3, Revision 0

Section 4OA5: Other Activities

Miscellaneous

INPO Letter, INPO Equipment Reliability Scram Review Visit, May 31, 2016

Root Cause Evaluation for CR-IP2-2016-00564

A-12

LIST OF ACRONYMS

10 CFR Title 10 of the Code of Federal Regulations

ADAMS Agencywide Document Access and Management System

ALARA as low as is reasonably achievable

AVR automatic voltage regulator

CAP corrective action program

CCW component cooling water

CR condition report

CVCS chemical and volume control system

EC engineering change

ECCS emergency core cooling system

EDG emergency diesel generator

GPI groundwater protection initiative

IASCC irradiation-assisted stress-corrosion cracking

IMC Inspection Manual Chapter

INPO Institute of Nuclear Power Operations

LER licensee event report

LOCA loss-of-coolant accident

MBFP main boiler feedwater pump

MCC motor control center

MOV motor operated valve

MRP materials reliability program

MW monitoring well

NCV non-cited violation

NRC Nuclear Regulatory Commission, U.S.

ODCM offsite dose calculation manual

OOS out of service

PAB primary auxiliary building

PFP pre-fire plan

RCS reactor coolant system

REMP radiological environmental monitoring program

RFO refueling outage

RW recovery well

SI safety injection

SSC structure, system, and component

TS technical specification

UFSAR updated final safety evaluation report

URI unresolved item

UT ultrasonic testing

WO work order