IR 05000321/2006003: Difference between revisions
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| issue date = 07/27/2006 | | issue date = 07/27/2006 | ||
| title = IR 05000321-06-003, 05000366-06-003 - Hatch Inspection Report 2006003 | | title = IR 05000321-06-003, 05000366-06-003 - Hatch Inspection Report 2006003 | ||
| author name = Shaeffer S | | author name = Shaeffer S | ||
| author affiliation = NRC/RGN-II/DRS | | author affiliation = NRC/RGN-II/DRS | ||
| addressee name = Stinson L | | addressee name = Stinson L | ||
| addressee affiliation = Southern Nuclear Operating Co, Inc | | addressee affiliation = Southern Nuclear Operating Co, Inc | ||
| docket = 05000321, 05000366 | | docket = 05000321, 05000366 | ||
| Line 18: | Line 18: | ||
=Text= | =Text= | ||
{{#Wiki_filter | {{#Wiki_filter:July 27, 2006Southern Nuclear Operating Company, Inc.ATTN: Mr. L. Vice President - Hatch ProjectP. O. Box 1295 Birmingham, AL 35201-1295SUBJECT:EDWIN I. HATCH NUCLEAR PLANT - NRC INTEGRATED INSPECTIONREPORT 05000321/2006003 AND 05000366/2006003 | ||
==Dear Mr. Stinson:== | ==Dear Mr. Stinson:== | ||
| Line 30: | Line 25: | ||
The inspectors reviewed selected procedures and records, observed activities, and interviewed personnel. Based on the results of this inspection, no findings of significance were identified.In accordance with 10 CFR 2.390 of the NRC's "Rules of Practice," a copy of this letter, itsenclosures, and your response (if any) will be available electronically for public inspection in theNRC Public Document Room or from the Publicly Available Records (PARS) component of theNRC's document system (ADAMS). ADAMS is accessible from the NRC Web site at http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room). | The inspectors reviewed selected procedures and records, observed activities, and interviewed personnel. Based on the results of this inspection, no findings of significance were identified.In accordance with 10 CFR 2.390 of the NRC's "Rules of Practice," a copy of this letter, itsenclosures, and your response (if any) will be available electronically for public inspection in theNRC Public Document Room or from the Publicly Available Records (PARS) component of theNRC's document system (ADAMS). ADAMS is accessible from the NRC Web site at http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room). | ||
Sincerely,/RA/Scott M. Shaeffer, ChiefReactor Projects Branch 2 Division of Reactor ProjectsDocket Nos. 50-321, 50-366License Nos. DPR-57 and NPF-5 | Sincerely, | ||
/RA/Scott M. Shaeffer, ChiefReactor Projects Branch 2 Division of Reactor ProjectsDocket Nos. 50-321, 50-366License Nos. DPR-57 and NPF-5 | |||
===Enclosure:=== | ===Enclosure:=== | ||
Inspection Report 05000321/2006003 and 05000366/2006003 | Inspection Report 05000321/2006003 and 05000366/2006003 w/Attachment: Supplemental Information | ||
REGION IIDocket Nos.:50-321, 50-366License Nos.:DPR-57 and NPF-5 Report Nos.:05000321/2006003 and 05000366/2006003 Licensee:Southern Nuclear Operating Company, Inc. | |||
Facility:Edwin I. Hatch Nuclear Plant Location:Baxley, Georgia 31515 Dates:April 1, 2006 - June 30, 2006 Inspectors:D. Simpkins, Senior Resident InspectorJ. Hickey, Resident Inspector C. Rapp, Senior Project Engineer R. Carrion, Project Engineer G. McCoy, Senior Resident Inspector - VogtleApproved by:Scott M. Shaeffer, ChiefReactor Projects Branch 2 Division of Reactor Projects Enclosure | Facility:Edwin I. Hatch Nuclear Plant Location:Baxley, Georgia 31515 Dates:April 1, 2006 - June 30, 2006 Inspectors:D. Simpkins, Senior Resident InspectorJ. Hickey, Resident Inspector C. Rapp, Senior Project Engineer R. Carrion, Project Engineer G. McCoy, Senior Resident Inspector - VogtleApproved by:Scott M. Shaeffer, ChiefReactor Projects Branch 2 Division of Reactor Projects Enclosure | ||
| Line 170: | Line 151: | ||
==LIST OF DOCUMENTS REVIEWED== | ==LIST OF DOCUMENTS REVIEWED== | ||
==Section 1R04: Equipment AlignmentS-5584B,== | ==Section 1R04: Equipment AlignmentS-5584B,== | ||
: PSW Strainer - Instruction Manual52PM-P41-035-0, PSW Strainer Maintenance | : PSW Strainer - Instruction Manual52PM-P41-035-0, PSW Strainer Maintenance | ||
}} | }} | ||
Revision as of 14:24, 13 July 2019
| ML062090010 | |
| Person / Time | |
|---|---|
| Site: | Hatch |
| Issue date: | 07/27/2006 |
| From: | Scott Shaeffer Division of Reactor Safety II |
| To: | Stinson L Southern Nuclear Operating Co |
| References | |
| IR-06-003 | |
| Download: ML062090010 (19) | |
Text
July 27, 2006Southern Nuclear Operating Company, Inc.ATTN: Mr. L. Vice President - Hatch ProjectP. O. Box 1295 Birmingham, AL 35201-1295SUBJECT:EDWIN I. HATCH NUCLEAR PLANT - NRC INTEGRATED INSPECTIONREPORT 05000321/2006003 AND 05000366/2006003
Dear Mr. Stinson:
On June 30, 2006, the U. S. Nuclear Regulatory Commission (NRC) completed an inspection atyour Edwin I. Hatch Nuclear Plant, Units 1 and 2. The enclosed integrated inspection report documents the inspection results, which were discussed on July 14, 2006, with Mr. Dennis Madison and other members of your staff.The inspection examined activities conducted under your license as they relate to safety andcompliance with the Commission's rules and regulations and with the conditions of your license.
The inspectors reviewed selected procedures and records, observed activities, and interviewed personnel. Based on the results of this inspection, no findings of significance were identified.In accordance with 10 CFR 2.390 of the NRC's "Rules of Practice," a copy of this letter, itsenclosures, and your response (if any) will be available electronically for public inspection in theNRC Public Document Room or from the Publicly Available Records (PARS) component of theNRC's document system (ADAMS). ADAMS is accessible from the NRC Web site at http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room).
Sincerely,
/RA/Scott M. Shaeffer, ChiefReactor Projects Branch 2 Division of Reactor ProjectsDocket Nos. 50-321, 50-366License Nos. DPR-57 and NPF-5
Enclosure:
Inspection Report 05000321/2006003 and 05000366/2006003 w/Attachment: Supplemental Information
REGION IIDocket Nos.:50-321, 50-366License Nos.:DPR-57 and NPF-5 Report Nos.:05000321/2006003 and 05000366/2006003 Licensee:Southern Nuclear Operating Company, Inc.
Facility:Edwin I. Hatch Nuclear Plant Location:Baxley, Georgia 31515 Dates:April 1, 2006 - June 30, 2006 Inspectors:D. Simpkins, Senior Resident InspectorJ. Hickey, Resident Inspector C. Rapp, Senior Project Engineer R. Carrion, Project Engineer G. McCoy, Senior Resident Inspector - VogtleApproved by:Scott M. Shaeffer, ChiefReactor Projects Branch 2 Division of Reactor Projects Enclosure
SUMMARY OF FINDINGS
IR 05000321/2006-003, 05000366/2006-003; 04/01/2006-06/30/2006; Edwin I. Hatch NuclearPlant, Units 1 and 2; Routine Integrated Report.The report covered a three-month period of inspection by two resident inspectors. The
NRC'sprogram for overseeing the safe operation of commercial nuclear power reactors is described in NUREG-1649, Reactor Oversight Process, Revision 3, dated July 2000.A.
NRC-Identified and Self-Revealing Findings
No findings of significance were identified.
B.Licensee-Identified Violations
None.
Enclosure
REPORT DETAILS
Summary of Plant StatusUnit 1 completed a refueling outage on April 3 and operated at or near 100% Rated ThermalPower (RTP) until May 1 when a fire on the main generator bus duct caused a load reduction and outage until May 4. The unit remained at 100% for the remainder of the reporting period.Unit 2 operated at or near 100% RTP except for a reactor trip on April 5. The unit was returnedto full power on April 7 and remained at 100% RTP through the end of the reporting period.1.REACTOR SAFETYCornerstones: Initiating Events, Mitigating Systems, and Barrier Integrity1R01Adverse Weathera.Inspection ScopeSeasonal Readiness Review. The inspectors performed a seasonal review of licenseehot weather preparations. The inspectors reviewed licensee procedure DI-OPS-56-0293 Hot Weather Operation, and walked down the completed portions of the procedures. In addition, the inspectors reviewed the Technical Specifications (TS), Final Safety Analysis Report (FSAR) and drawings D-11001,11004, H-21033, 21039 to verify the following two systems would remain operable during hot weather.*Plant Service Water (PSW) system*Residual Heat Removal Service Water (RHRSW) systemImminent Adverse Weather. The inspectors also reviewed licensee actions in responseto a high winds on June 12. The inspectors reviewed licensee procedure 34AB-Y22-002-0, Abnormal Phenomena, and walked down external plant areas to ensure debris and loose materials were controlled to limit missile hazards especially near the switchyards and safety-related equipment.b.FindingsNo findings of significance were identified.
1R04 Equipment Alignmenta.Inspection ScopePartial Walkdowns.
The inspectors performed partial walkdowns of the following threesystems when the opposite trains were removed from service. The inspectors checkedsystem valve positions, electrical breaker positions, and operating switch positions toevaluate the operability of the opposite trains or components by comparing the positionlisted in the system operating procedure to the actual position. Documents reviewed arelisted in the Attachment.
4Enclosure*2C Emergency Diesel Generator (EDG) during 2A EDG maintenance*1A/1C EDGs during 1B EDG maintenance
- 2A/2C EDGs during 1B EDG maintenanceComplete Walkdown. The inspectors performed a complete walkdown of the followingsystem. The inspectors performed a detailed check of valve positions, electrical breaker positions, and operating switch positions to evaluate the operability of the r edundanttrains or components by comparing the required position in the system operatingprocedure to the actual position. The inspectors also interviewed personnel and reviewed control room logs to verify that alignment and equipment discrepancies were being identified and appropriately resolved. Documents reviewed are listed in the
.*Unit 1 PSW Systemb.FindingsNo findings of significance were identified.
1R05 Fire Protectiona.Inspection ScopeFire Area Tours.
The inspectors toured the following 12 risk significant plant areas toverify transient combustibles were being controlled in accordance with administrative procedures and the physical condition of fire detection devices was assessed to identify damage or obstructions which could affect functionality. Water based suppression systems were inspected to verify sprinkler heads and nozzles were not obstructed byoverhead equipment and major water supply valves were in the correct position. The inspectors reviewed the Fire Hazards Analysis drawings H-11846 and H-11847 to verify that the necessary fire fighting equipment, such as fire extinguishers, hose stations, ladders, and communications equipment, were in place. Documents reviewed are listed in the Attachment.*DC Switchgear Rooms*Transformer Rooms
- Low Pressure Coolant Injection Inverter Room
- Control Room
- Control Room Roof
- Unit 1 SE Residual Heat Removal (RHR) and Core Spray Room*Unit 1 Reactor Core Isolation Cooling (RCIC) Pump and Turbine Room
- Unit 1 NE RHR and Core Spray Room*Unit 1 Control Rod Drive (CRD) and DRW Sump Room*Unit 1 High Pressure Core Injection (HPCI) Room
- Unit 1 CRD Area
- Unit 1 Working Floor and Motor Generator Set Roomsb.FindingsNo findings of significance were identified.
5Enclosure1R06 Flood Protection Measuresa.Inspection ScopeInternal Flooding. The inspectors reviewed the FSAR and the individual plantexamination to determine the plant areas that were susceptible to internal floodingevents. The inspectors performed a detailed walkdown of the following area to determine potential sources of internal flooding and the condition of penetrations and sumps in the rooms. *Unit 1 Southwest Diagonal Switchgear Room *Unit 1 RCIC Pump RoomExternal Flooding. The inspectors reviewed the FSAR and Individual Plant Examinationfor plant design features that protect against external flooding and licensee procedure 10AC-MGR-013-00, Inclement Weather Policies, to verify the licensee's flood mitigation plans and equipment were consistent with the design requirements and risk analysis assumptions. The inspectors reviewed the material condition of flood protection barriers and exterior walls to verify they would perform their intended function.b.FindingsNo findings of significance were identified.
1R11 Licensed Operator Requalificationa.Inspection ScopeResident Quarterly Observation.
The inspectors observed the performance of licenseesimulator scenario LT-SG-50352-14 which included a loss of the Baxley Loop, forced load reduction, loss of the 2A Instrument Bus, Condensate System leak, Reactor Scram, Main Steam Isolation Valve closure, RCIC failure to auto start, and a HPCI turbine control valve malfunction. The inspectors reviewed licensee procedures 10AC-MGR-019-0S, Procedure Use and Adherence, and DI-OPS-59-0896N, Operations Management Expectations, to verify formality of communication, procedure usage, alarm response, control board manipulations, group dynamics, and supervisory oversight. The inspectors attended the post-exercise critique of operator performance to assess if the licensee identified performance issues were comparable to those identified by the inspectors. In addition, the inspectors reviewed the critique results from previous training sessions to assess performance improvement.b.FindingsNo findings of significance were identified.
6Enclosure1R12Maintenance Effectivenessa.Inspection ScopeThe inspectors reviewed the following two maintenance activities associated withstructures, systems, and components to assess the licensee's implementation of theMaintenance Rule (10 CFR 50.65) with respect to the characterization of failures and the appropriateness of the associated (a)(1) or (a)(2) classification. The inspectors also reviewed operator logs, Condition Reports (CRs), Maintenance Work Orders (MWOs)and the licensee's Maintenance Rule implementing procedures to determine if equipment failures were being identified, properly assessed, and corrective actions established to return the equipment to a satisfactory condition. Documents reviewed are listed in the Attachment.*Unit 2 Core Spray System*Unit 1 Analog Trip and Transmitter Systemb.FindingsNo findings of significance were identified.
1R13 Maintenance Risk Assessments and Emergent Work Evaluationa.Inspection ScopeThe inspectors reviewed the following five Plan of the Day (POD) documents listedbelow to verify that risk assessments were performed prior to components being
removed from service. The inspectors reviewed the risk assessment and risk management controls implemented for these activities to verify they were completed in accordance with licensee procedure 90AC-OAM-002-0, Scheduling Maintenance, and 10 CFR 50.65 (a)(4). For emergent work, the inspectors assessed whether any increase in risk was promptly assessed and that appropriate risk management actions were implemented.*POD for Week of 4/15-21*POD for Week of 4/22-28
- POD for Week of 4/29-5/5
- POD for Week of 5/20-26
- POD for Week of 6/24-30b.FindingsNo findings of significance were identified.
7Enclosure1R14Personnel Performance During Non-routine Plant Evolutionsa.Inspection ScopeFor the two events described below, the inspectors observed operator actions andreviewed operator logs and computer data to verify proper operator actions were taken.
Documents reviewed are listed in the Attachment.*Unit 2 Scram due to MVAR recorder calibration*Notification of Unusual Event declared for a Unit 1 Isophase Bus Duct Fireb.FindingsNo findings of significance were identified.
1R15 Operability Evaluationsa.Inspection ScopeThe inspectors reviewed the following five operability evaluations and compared theevaluations to t
he system requirements identified in the TSs and the FSAR to ensurethat operability was adequately assessed and the system or component remainedavailable to perform it's intended function. Also, the inspectors assessed the adequacy of compensatory measures implemented as a result of the condition. Documents reviewed are listed in the Attachment.*Unit 1 Local Power Range Monitor gain adjustment factors greater than acceptancecriteria*Unit 1 1F Safety Relief Valve (SRV) elevated tailpipe temperature
- Unit 1 SRV Quick Disconnect fittings not aligned per designb.FindingsNo findings of significance were identified.
1R19 Post-Maintenance Testinga.Inspection ScopeFor the following five post-maintenance tests, the inspectors reviewed the test scope toverify the test demonstrated the work performed was completed correctly and the
affected equipment was functional and operable in accordance with TS requirements.
Following the maintenance activities, the inspectors reviewed equipment status and alignment to verify the system or component was available to perform the requiredsafety function. Documents reviewed are listed in the Attachment.
8Enclosure*1E41F036, HPCI Steam Trap Inlet Isolation Valve repack*1P41D106A, RHRSW Pump A cooling water flow indicator replacement*2E41F005, HPCI Discharge Check Valve Bonnet Seal leak
- 1E51F017, RCIC Suction Relief Valve removal/test/installb.FindingsNo findings of significance were identified.
1R20 Refueling and Outage Activitiesa.Inspection ScopeThe inspectors witnessed the Unit 1 and Unit 2 plant start up.
The inspectors reviewedplant configurations, technical specifications, license conditions and administrative procedure prerequisites for pending mode changes. Documents reviewed are listed in the Attachment.b.FindingsNo findings of significance were identified.
1R22 Surveillance Testinga.Inspection ScopeThe inspectors reviewed licensee surveillance test procedures and either witnessed thetest or reviewed test records for the following six surveillances to determine if the scope
of the test adequately demonstrated the affected equipment was operable. The inspectors reviewed these activities to assess for preconditioning of equipment, procedure adherence, and equipment alignment following completion of the surveillance. The inspectors reviewed licensee procedure AG-MGR-21-0386N, Evolution and Pre- and Post-Job Brief Guidance, and attended selected briefings to determine if procedure requirements were met. Documents reviewed are listed in the
.Surveillance Tests*34SV-R43-011-2, Diesel Generator 2A 24 Month Operability Test*34SV-R43-006-2, Diesel Generator 2C Sem-Annual Test
- 34SV-C71-004-2, Manual Scram Functional Test
- 42IT-TET-020-0, Control Room Inleakage Tracer Gas TestIn-Service Test*34SV-E41-001-1, RCIC Operability UnitReactor Coolant System (RCS) Leakage Detection*34SV-SUV-019-1, Surveillance Checks 9Enclosureb.FindingsNo findings of significance were identified.
1R23 Temporary Plant Modificationsa.Inspection ScopeThe inspectors reviewed the following temporary modification (TMM) and assessed theevaluation using criteria defined in licensee procedure 40AC-ENG-018-0S, Temporary
Modification Control. In addition, the 10 CFR 50.59 evaluation was assessed using the design basis information provided in the FSAR to verify the modification did not affect the safety functions of this system. The inspectors also verified the modification wasinstalled in accordance with the TMM requirements.*TMM 2-06-015, Bypassing of one Unit 2 Turbine Building leak detector (TemperatureSensor)b.FindingsNo findings of significance were identified.1EP6Drill Evaluationa.Inspection ScopeThe inspectors observed the following two emergency plan evolutions. The inspectorsobserved licensee activities in the simulator, Technical Support Center and Operations Support Center to verify implementation of licensee procedure 10AC-MGR-006-0, Hatch Emergency Plan. The inspectors reviewed the classification of the simulated events and the development of protective action recommendations to verify these activities were conducted in accordance with licensee procedure 73EP-EIP-001-0, Emergency Classification and Initial Actions. The inspectors also reviewed licensee procedure 73EP-EIP-073-0, Onsite Emergency Notification, to verify the proper offsite notifications were made. The inspectors attended the post-exercise critique to assess the licensee's effectiveness in identifying areas of improvement. Documents reviewed are listed in the
.*Emergency Plan Drill conducted on May 17*Simulator Education Drill on J une 14b.FindingsNo findings of significance were identified.
10Enclosure4.OTHER ACTIVITIES4OA1Performance Indicator Verification
a. Inspection Scope
The inspectors reviewed a sample of the licensee submittals for the performanceindicators (PIs) listed below to verify the accuracy of the data reported. The PI definitions and the guidance contained in NEI 99-02, Regulatory Assessment Indicator Guideline, Rev. 2 and licensee procedure 00AC-REG-005-0S, preparation and reporting of NRC PI Data, were used to verify procedure and reporting requirements were met.Initiating Events Cornerstone*Unit 1 and 2 Reactor Coolant System Leakage*Unit 1 and 2 Reactor Coolant System ActivityThe inspectors reviewed raw PI data collected from July 2004 through March 2006 forthe RCS leakage indicators and from June 2004 through March 2006 for the RCS activity indicators and compared graphical and tabular representations from the most recent PI report to the raw data to verify that the data was included in the report. Theinspectors also examined a sampling of operations logs and procedures to verify the PI data was appropriately captured for inclusion into the PI report, and the individual PIs were calculated correctly. Documents reviewed are listed in the Attachment.
b. Findings
No findings of significance were identified.4OA2Identification and Resolution of Problems.1Daily Screening of Corrective Action ItemsAs required by Inspection Procedure 71152, Identification and Resolution of Problems, andin order to help identify repetitive equipment failures or specific human performance issues for follow-up, the inspectors performed a daily screening of items entered into the licensee's corrective action program. This review was accomplished by either attending daily screening meetings that briefly discussed major CRs, or accessing the licensee's computerized corrective action database and reviewing each CR that was initiated..2Semi-Annual Trend Reviewa.Inspection ScopeThe inspectors performed a review of the licensee's Corrective Action Program andassociated documents to identify trends which could indicate the existence of a more significant safety issue. The review was focused on repetitive equipment issues, but also considered the results of inspector daily CR screening, licensee trending efforts, 11Enclosureand licensee human performance results. The review nominally considered the sixmonth period of January 2006 through June 2006 although some examples extended beyond those dates when the scope of the trend warranted. The inspectors also reviewed several CRs associated with operability determinations which occurred duringthe period. The inspectors compared and contrasted their results with the results contained in the licensees two latest quarterly trend reports. Corrective actions associated with a sample of the issues identified in the licensee's trend reports were reviewed for adequacy. The inspectors also evaluated the trend reports against the requirements of the licensee's corrective action program as specified in licensee procedure NMP-GM-002, Corrective Action Program, and 10 CFR 50, Appendix B.
Documents reviewed are listed in the Attachment.b.Findings and ObservationsNo findings of significance were identified. The inspectors compared the licenseeQuarterly Trend Report with the results of the inspectors' daily CR screening and did not identify any discrepancies or potential trends in the data that the licensee had failed toidentify. 4OA3Event Followup.1(Closed) LER 05000321/2004-001, Residual Heat Removal Service Water Pump Inoperablefor Failure to meet NPSH RequirementsOn February 3, 2004, an evaluation revealed that the Net Positive Suction Head requirements for the 1C RHRSW Pump were not met when river level fell below 65.9 feetfrom September 14, 2003 through November 17, 2003. On December 12, 2003 the 1C RHRSW Pump was replaced and successfully tested. This condition was documented in CR2003112330. No findings of significance were identified..2(Closed) LER 05000321/2004-005, Degraded Motor Generator Set Results in ReactorProtection System Bus TripOn April 15, 2004, the "B" Reactor Protection System Motor Generator Set tripped. As aresult, several primary containment isolation valves repositioned to the fail-safe position of closed due to a loss of power. The degraded motor was replaced with a new motor. This condition was documented in CR 2004104570. No findings of significance were identified..3(Closed) LER 05000366/2004-003, Failure to Restore Caution Tag on Service Air SystemResulted in Primary Containment InoperabilityOn October 3, 2004, primary containment was declared inoperable because both penetration22 manual isolation valves were open. One of the affected valves was subsequently closed, which restored primary containment to operable status. A Caution Tag clearance had not been properly restored prior to changing modes. This condition was documented in CR 2004109710. No findings of significance were identified.
12Enclosure4OA5Other.1(Closed) NRC Temporary Instruction (TI) 2515/165: Operational Readiness of Offsite Powerand Impact on Plant RiskThe inspectors reviewed licensee procedures and controls and interviewed operations andmaintenance personnel to verify these documents contained specific attributes delineated in the TI to ensure the operational readiness of offsite power systems in accordance with plantTechnical Specifications; the design requirements provided in 10 CFR 50, Appendix A, General Design Criterion 17, Electric Power Systems; and the impact of maintenance on plant risk in accordance with 10 CFR 50.65(a)(4), Requirements for Monitoring the Effectiveness of Maintenance at Nuclear Power Plants. Appropriate documentation of the results of this inspection was provided to NRC headquarters staff for further analysis, asrequired by the TI. This completes the Region II inspection TI requirements for the Hatch Nuclear Plant.4OA6Meetings, Including Exit.1Exit MeetingOn July 14, the inspectors presented the inspection results to Mr. Dennis Madison and othermembers of his staff who acknowledged the findings. The inspectors confirmed that all proprietary information examined during the inspection was controlled in accordance with appropriate guidelines.ATTACHMENT:
SUPPLEMENTAL INFORMATION
KEY POINTS OF CONTACT
Licensee personnel
- M. Ajluni, Assistant General Manager - Plant Support
- J. Dixon, Health Physics Manager
- S. Douglas, Assistant General Manager - Plant Operations
- M. Googe, Maintenance Manager
- J. Hammonds, Operations Manager
- J. Lewis, Training and Emergency Preparedness Manager
- D. Madison, General Manager - Nuclear Plant
- J. Thompson, Nuclear Security Manager
- R. Varnadore, Engineering Manager
NRC personnel
- S. Shaeffer, Chief, Region II Reactor Project Branch 2
LIST OF ITEMS OPENED, CLOSED, AND DISCUSSED
Closed05000321/2004-001LER Residual Heat Removal Service Water Pump Inoperablefor Failure to meet NPSH Requirements (Section 4OA3.1)05000321/2004-005LER Degraded Motor Generator Set Results in ReactorProtection System Bus Trip (Section 4OA3.2)05000366/2004-003LERFailure to Restore Caution Tag on Service Air SystemResulted in Primary Containment Inoperability (Section
4OA3.3)2515/165TI Operational Readiness of Offsite Power and Impact onPlant Risk (Section 4OA5)
LIST OF DOCUMENTS REVIEWED
Section 1R04: Equipment AlignmentS-5584B,
- PSW Strainer - Instruction Manual52PM-P41-035-0, PSW Strainer Maintenance