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| number = ML17332A260
| number = ML17332A260
| issue date = 08/19/1994
| issue date = 08/19/1994
| title = Responds to NRC 940720 Ltr Re Violation Noted in Insp Repts 50-315/94-13 & 50-316/94-13.Corrective Actions:Work Control Process Code Was Changed on 2-MMO-240 Repair Job Order & CAP PMI-7030 Will Be Revised to Redefine Rework
| title = Responds to NRC Re Violation Noted in Insp Repts 50-315/94-13 & 50-316/94-13.Corrective Actions:Work Control Process Code Was Changed on 2-MMO-240 Repair Job Order & CAP PMI-7030 Will Be Revised to Redefine Rework
| author name = FITZPATRICK E
| author name = Fitzpatrick E
| author affiliation = INDIANA MICHIGAN POWER CO. (FORMERLY INDIANA & MICHIG
| author affiliation = INDIANA MICHIGAN POWER CO. (FORMERLY INDIANA & MICHIG
| addressee name = MARTIN J B
| addressee name = Martin J
| addressee affiliation = NRC OFFICE OF INFORMATION RESOURCES MANAGEMENT (IRM)
| addressee affiliation = NRC OFFICE OF INFORMATION RESOURCES MANAGEMENT (IRM)
| docket = 05000315, 05000316
| docket = 05000315, 05000316
Line 11: Line 11:
| contact person =  
| contact person =  
| document report number = AEP:NRC:1212G, NUDOCS 9408240071
| document report number = AEP:NRC:1212G, NUDOCS 9408240071
| title reference date = 07-20-1994
| document type = CORRESPONDENCE-LETTERS, INCOMING CORRESPONDENCE
| document type = CORRESPONDENCE-LETTERS, INCOMING CORRESPONDENCE
| page count = 10
| page count = 10
}}
}}
See also: [[followed by::IR 05000315/1994013]]


=Text=
=Text=
{{#Wiki_filter:(ACCELERATED
{{#Wiki_filter:(ACCELERATED RIDS PROCESSING)
RIDS PROCESSING)
REGULATORY INFORMATION DISTRIBUTION SYSTEM (RIDS)
R EGULATORY INFORMATION
'CESSION NBR:9408240071 DOC.DATE: 94/08/19 NOTARIZED: YES DOCKET FACIL:50-315 Donald C.
DISTRIBUTION
Cook Nuclear Power Plant, Unit 1, Indiana M
SYSTEM (RIDS)'CESSION NBR:9408240071
05000315 50-316 Donald C.
DOC.DATE: 94/08/19 NOTARIZED:
Cook Nuclear Power Plant, Unit 2, Indiana M
YES DOCKET FACIL:50-315
05000316 AUTH.NAME AUTHOR AFFILIATION FITZPATRICK,E.
Donald C.Cook Nuclear Power Plant, Unit 1, Indiana M 05000315 50-316 Donald C.Cook Nuclear Power Plant, Unit 2, Indiana M 05000316 AUTH.NAME AUTHOR AFFILIATION
Indiana Michigan Power Co.
FITZPATRICK,E.
(formerly Indiana
Indiana Michigan Power Co.(formerly Indiana&Michigan Ele RECIP.NAME
& Michigan Ele RECIP.NAME RECIPIENT AFFILIATION Document Control Branch (Document Control Desk)
RECIPIENT AFFILIATION
 
Document Control Branch (Document Control Desk)SUBJECT: Responds to NRC 940720 ltr re violations
==SUBJECT:==
noted in insp rept 50-315/94-13
Responds to NRC 940720 ltr re violations noted in insp rept 50-315/94-13
&50-316/94-13.Corrective
& 50-316/94-13.Corrective actions:work control process code was changed on 2-MMO-240 repair job order PMI-7030 will be revised to redefine rework.
actions:work
DISTRIBUTION CODE:
control process code was changed on 2-MMO-240 repair job order&PMI-7030 will be revised to redefine rework.DISTRIBUTION
IE01D COPIES RECEIVED:LTR ENCL SIZE:
CODE: IE01D COPIES RECEIVED:LTR
TITLE: General (50 Dkt)-Insp Rept/Notice of Vio ation Response NOTES:
ENCL SIZE: TITLE: General (50 Dkt)-Insp Rept/Notice
RECIPIENT ID CODE/NAME PD3-1 PD INTERNAL: AEOD/DEIB AEOD/S PD/RRAB DEDRO NRR/DRCH/HHFB, NUDOCS-ABSTRACT OGC/HDS2 RES/HFB EXTERNAL EG &G/ BRYCE i J
of Vio ation Response NOTES: RECIPIENT ID CODE/NAME PD3-1 PD INTERNAL: AEOD/DE I B AEOD/S PD/RRAB DEDRO NRR/DRCH/HHFB, NUDOCS-ABSTRACT
~ H ~
OGC/HDS2 RES/HFB EXTERNAL EG&G/BRYCE i J~H~NRC PDR COPIES LTTR ENCL 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 RECIPIENT ID CODE/NAME HICKMAN,J AEOD/SPD/RAB
NRC PDR COPIES LTTR ENCL 1
AEOD/TTC NRR/DORS/OEAB
1 1
NRR/PMAS/IRCB-E
1 1
0 R REG FIL 02 GN3 FILE 01 NOAC COPIES LTTR ENCL 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 NOTE TO ALL"RIDS" RECIPIENTS:
1 1
PLEASE HELP US TO REDUCE iVASTE!CONTACT THE DOCUMENT CONTROL DESK, ROOM Pl-37 (EXT.504-2083)TO ELIMINATE YOUR NAME F ROTI DISTRIBUTION
1 1
LISTS FOR DOCUMENTS YOU DON"I'EED!TOTAL NUMBER OF COPIES REQUIRED'TTR
1 1
19 ENCL 19  
1 1
1 1
Indiana Michigan Power Company P.O.Box 16631 Columbus, OH 43216 INDIANA NICHIGAN POWER AEP;NRC'1212G
1 1
10 CFR 2.201 Donald C.Cook Nuclear Plant Units 1 and 2 Docket Nos.50-315 and 50-316 License Nos.DPR-58 and DPR-74 NRC INSPECTION
1 1
REPORTS NO.50-315/94013 (DRP)AND 50-316/94013 (DRP)REPLY TO NOTICE OF VIOLATION U.S.Nuclear Regulatory
1 RECIPIENT ID CODE/NAME HICKMAN,J AEOD/SPD/RAB AEOD/TTC NRR/DORS/OEAB NRR/PMAS/IRCB-E 0
Commission
R REG FIL 02 GN3 FILE 01 NOAC COPIES LTTR ENCL 1
Document Control Desk Washington, D.C.20555 Attn: Mr.J.B.Martin August 19, 1994 Dear Mr.Martin: This letter is in response to a USNRC letter dated July 20, 1994, that forwarded a notice of violation to Indiana Michigan Power Company.The notice of violation contained one violation identified
1 1
during a routine safety inspection
1 1
conducted by Messrs.J.A.Isom, D.J.Hartland, and D.L.Shepard from June 4, 1994, through July 1, 1994.The violation is associated
1 1
with the repeated packing failures of a Unit 2 main steam test selector valve over a period of two years that resulted in several entries into four-hour limiting conditions
1 1
of operation.
1 1
Our reply to the notice of violation is provided in the attachment
1 1
to this letter.This letter is submitted pursuant to 10 CFR 50.54(f)and, as such, an oath statement is attached.p~W)Vice President ar Attachment
1 1
940S240071
1 1
94081 PDR ADDCI;05000315 PDFi'gy/  
1 NOTE TO ALL"RIDS" RECIPIENTS:
Mr.J.B.Martin-2-AEP:NRC:1212G
PLEASE HELP US TO REDUCE iVASTE!CONTACTTHE DOCUMENTCONTROL DESK, ROOM Pl-37 (EXT. 504-2083 ) TO ELIMINATEYOUR NAME F ROTI DISTRIBUTIONLISTS FOR DOCUMENTS YOU DON"I'EED!
CC: A.A.Blind G.Charnoff W.T.Russell, NRC-Washington, D.C.NRC Resident Inspector NFEM Section Chief J.R.Padgett  
TOTAL NUMBER OF COPIES REQUIRED'TTR 19 ENCL 19
STATE OF OHIO COUNTY OF FRANKLIN E.E.Fitzpatrick, being duly sworn, deposes and says that he is the Vice President of licensee Indiana Michigan Power Company, that he has read the foregoing response to NRC INSPECTION
 
REPORTS NO.50-315/94013 (DRP)AND 50-316/94013 (DRP), REPLY TO NOTICE OF VIOLATION and knows the contents thereof;and that said contents are true to the best of his knowledge and belief.Subscribed
Indiana Michigan Power Company P.O. Box 16631 Columbus, OH 43216 INDIANA NICHIGAN POWER AEP;NRC'1212G 10 CFR 2.201 Donald C.
end sworn to before me this~PE day of 19~EX NOTARY PUBLIC Ale D.HILL gpgpy pUQUC, STAIE pF plllp SSX SSh',IEISSISS
Cook Nuclear Plant Units 1 and 2
EXPIRES~  
Docket Nos.
ATTACHMENT
50-315 and 50-316 License Nos.
TO AEP:NRC:1212G
DPR-58 and DPR-74 NRC INSPECTION REPORTS NO. 50-315/94013 (DRP)
REPLY TO NOTICE OF VIOLATION  
AND 50-316/94013 (DRP)
ATTACHMENT
REPLY TO NOTICE OF VIOLATION U.
TO AEP:NRC:1212G
S. Nuclear Regulatory Commission Document Control Desk Washington, D.
Page 1 Background
C.
A routine safety inspection
20555 Attn:
was conducted by Messrs.James A.Isom, David J.Hartland, and Douglas L.Shepard from Jurie 4, 1994, through July 1, 1994.During this inspection, one item was found to be in violation.
Mr. J.
The violation was identified
B. Martin August 19, 1994
as the failure to correct che root cause for the repeated packing failures of a Unit 2 main steam test selector valve over a period of two years that resulted in several entries into four-hour limiting conditions
 
of operation.
==Dear Mr. Martin:==
This violation was set forth in a letter containing
This letter is in response to a USNRC letter dated July 20,
the notice of violation, dated July 20, 1994, fromMr.E.G.Greenman, Director, Division of Reactor Projects, USNRC, Region III.The letter was received July 25, 1994.Our response to the notice of violation is contained within this document.NRC Violation"10 CFR 50, Appendix B, Criterion XVI,"Corrective
: 1994, that forwarded a notice of violation to Indiana Michigan Power Company.
Action," requires in part that"Measures shall be established
The notice of violation contained one violation identified during a
to assure that conditions
routine safety inspection conducted by Messrs. J.
adverse to quality are promptly identified
A. Isom, D. J. Hartland, and D. L. Shepard from June 4,
and corrected.
: 1994, through July 1, 1994.
In the case of significant
The violation is associated with the repeated packing failures of a Unit 2 main steam test selector valve over a period of two years that resulted in several entries into four-hour limiting conditions of operation.
conditions
Our reply to the notice of violation is provided in the attachment to this letter.
adverse to quality, the measures shall assure that the cause of the condition is determined
This letter is submitted pursuant to 10 CFR 50.54(f) and, as such, an oath statement is attached.
and corrective
p~W)
action taken to preclude repetition." Contrary to the above, as of July 1, 1994, the licensee failed to replace the pitted valve stem on main steam stop valve (MSSV)dump valve test selector, 2-MM0-240, a significant
Vice President ar Attachment 940S240071 94081 PDR ADDCI; 05000315PDFi'gy
condition adverse to quality.Specifically, Action Request 25594 had been written on July 8,'992, to replace the pitted valve stem but was not scheduled to be performed until the refueling outage starting in September 1994.Consequently, 2-MMO-240 had to be repacked five times, requiring entries into the four hour Limiting Condition of Operation (LCO), as required by Technical Specification (TS)4.7.1.5.1.
/
There were several opportunities
 
since July 1992 to replace the stem without entering the LCO.This is a Severity Level IV violation (Supplement
Mr. J.
I).  
B. Martin AEP:NRC:1212G CC:
ATTACHMENT
A. A. Blind G. Charnoff W. T. Russell, NRC - Washington, D.C.
TO AEP:NRC: 1212G Page 2 Response to Violation dmissio or Denial o the Alle ed Violat o Indiana Michigan Power Company admits to the violation as cited in the NRC notice of violation.
NRC Resident Inspector NFEM Section Chief J.
2.easons for the Violatio The root cause for this violation has been identified
R. Padgett
as a programmatic
 
weakness in the plant's corrective
STATE OF OHIO COUNTY OF FRANKLIN E.
action program.In July 1992, Unit 2 was in Mode 3 (Hot Standby).While repacking 2-MM0-240, the valve stem was found to be pitted, scored and in need of replacement.
E. Fitzpatrick, being duly sworn, deposes and says that he is the Vice President of licensee Indiana Michigan Power
At that time an Action Request was initiated to replace the stem.Since a repair activity of this type requires cooldown to Mode 5 to perform, a scheduling
: Company, that he has read the foregoing response to NRC INSPECTION REPORTS NO. 50-315/94013 (DRP)
code of U2R94 was assigned, adding the repair to the scope of the 1994 refueling outage.At the time the U2R94 code was assigned, in the absence of prior failure history, this was the correct designation.
AND 50-316/94013 (DRP),
The valve stem replacement
REPLY TO NOTICE OF VIOLATION and knows the contents thereof; and that said contents are true to the best of his knowledge and belief.
would only have been elevated to the forced outage schedule if the subsequent, repeated repairs had been identified
Subscribed end sworn to before me this ~PE day of 19~EX NOTARY PUBLIC Ale D. HILL gpgpy pUQUC, STAIE pF plllp SSX SSh',IEISSISS EXPIRES~
as rework and an adverse trend.Since the valve stem deficiency
 
was first identified, 2-MMO-240 has been repacked five additional
ATTACHMENT TO AEP:NRC:1212G REPLY TO NOTICE OF VIOLATION
times.Had the valve stem replacement
 
been scheduled as a forced outage activity, there would have been two opportunities
ATTACHMENT TO AEP:NRC:1212G Page
prior to the violation to complete the repair.The first opportunity
 
occurred in August 1993 when the unit experienced
===1 Background===
a reactor trip and forced outage.The second opportunity
A routine safety inspection was conducted by Messrs.
occurred in January 1994 when the unit was removed from service to repair an unisolable
James A. Isom, David J. Hartland, and Douglas L. Shepard from Jurie 4, 1994, through July 1, 1994.
steam leak on Steam Generator 21 blowdown line.Repeated packing replacements
During this inspection, one item was found to be in violation.
were not identified
The violation was identified as the failure to correct che root cause for the repeated packing failures of a Unit 2 main steam test selector valve over a period of two years that resulted in several entries into four-hour limiting conditions of operation.
in the plant's Corrective
This violation was set forth in a letter containing the notice of violation, dated July 20, 1994, fromMr. E.
Action Program (PMI-7030)
G. Greenman, Director, Division of Reactor Projects, USNRC, Region III.
as an adverse trend.PMI-7030,"Corrective
The letter was received July 25, 1994.
Action Program," requires a condition report to be written for similar corrective
Our response to the notice of violation is contained within this document.
maintenance
NRC Violation "10 CFR 50, Appendix B, Criterion XVI, "Corrective Action,"
work within 90 days of the original deficiency.
requires in part that "Measures shall be established to assure that conditions adverse to quality are promptly identified and corrected.
Only the final packing failure on May 17, 1994, fell within the 90 day criteria, as this failure occurred 57 days after the previous repair on March 21, 1994.  
In the case of significant conditions adverse to quality, the measures shall assure that the cause of the condition is determined and corrective action taken to preclude repetition."
ATTACHMENT
Contrary to the
TO AEP:NRC: 12120 Page 3 A rework condition report was not initiated following the May 17 failure due to an error in the Maintenance
: above, as of July 1, 1994, the licensee failed to replace the pitted valve stem on main steam stop valve (MSSV) dump valve test
Administrative
: selector, 2-MM0-240, a
Procedure (MAP)¹MA3.3-05,"Maintenance
significant condition adverse to quality.
Planning".
Specifically, Action Request 25594 had been written on July 8,'992, to replace the pitted valve stem but was not scheduled to be performed until the refueling outage starting in September 1994.
MAP¹MA3.3-05 incorrectly
Consequently, 2-MMO-240 had to be repacked five times, requiring entries into the four hour Limiting Condition of Operation (LCO),
defined rework as similar work performed within 30 days of the original failure, rather than 90 days.As a result of this error the maintenance
as required by Technical Specification (TS) 4.7.1.5.1.
planner failed to identify the reoccurrence
There were several opportunities since July 1992 to replace the stem without entering the LCO.
of the packing leak on May 17, 1994, as falling within the definition
This is a Severity Level IV violation (Supplement I).
of rework.3.Cor ective Actions Taken and esults eyed The work control process code was changed on the 2-MMO-240 repair Job Order.The 2-MMO-240 repair task now appears on the forced outage schedule, as well as within the scope of the refueling outage.MAP¹MA3.3-05,"Maintenance
 
Planning," was revised to reflect the current definition
ATTACHMENT TO AEP:NRC: 1212G Page 2
of rework contained in PMI-7030.4.Corrective
 
Actions Taken to Avoid Further Violations
===Response===
PMI-7030,"Corrective
to Violation dmissio or Denial o the Alle ed Violat o Indiana Michigan Power Company admits to the violation as cited in the NRC notice of violation.
Action," will be revised to redefine rework.The definition
2.
for rework will now include any corrective
easons for the Violatio The root cause for this violation has been identified as a
maintenance
programmatic weakness in the plant's corrective action program.
which requires entry into a Limiting Condition of Operation (LCO)if similar work has been performed on that equipment/component
In July 1992, Unit 2 was in Mode 3 (Hot Standby).
during the current operating cycle, including the previous refueling outage.When rework of this type occurs, a Condition Report will be written to aid in the identification/evaluation
While repacking 2-MM0-240, the valve stem was found to be pitted, scored and in need of replacement.
of an adverse trend.The"90-day" standard will be retained for work upon equipment or components
At that time an Action Request was initiated to replace the stem.
which do not initiate an LCO entry.MAP¹MA3.3-05,"Maintenance
Since a repair activity of this type requires cooldown to Mode 5
Planning," will be revised to refer to PMI-7030 for the above-described
to perform, a scheduling code of U2R94 was assigned, adding the repair to the scope of the 1994 refueling outage.
redefinition
At the time the U2R94 code was assigned, in the absence of prior failure history, this was the correct designation.
of rework.These measures will assure that this type of condition will be precluded in the future.5.ate When Full Com lienee Will Be Achieved PMI-7030 and MAP modifications
The valve stem replacement would only have been elevated to the forced outage schedule if the subsequent, repeated repairs had been identified as rework and an adverse trend.
will be completed by September 30, 1994.  
Since the valve stem deficiency was first identified, 2-MMO-240 has been repacked five additional times.
ATTACHMENT
Had the valve stem replacement been scheduled as a forced outage activity, there would have been two opportunities prior to the violation to complete the repair.
TO AEP:NRC:1212G
The first opportunity occurred in August 1993 when the unit experienced a reactor trip and forced outage.
Page 4 The valve stem replacement
The second opportunity occurred in January 1994 when the unit was removed from service to repair an unisolable steam leak on Steam Generator 21 blowdown line.
for 2-MMO-240 will be completed during the first Mode 5 forced outage of sufficient
Repeated packing replacements were not identified in the plant's Corrective Action Program (PMI-7030) as an adverse trend.
duration or the upcoming Unit 2 refueling outage, scheduled to commence September 6, 1994, whichever occurs first.
PMI-7030, "Corrective Action Program,"
}}
requires a
condition report to be written for similar corrective maintenance work within 90 days of the original deficiency.
Only the final packing failure on May 17, 1994, fell within the 90 day criteria, as this failure occurred 57 days after the previous repair on March 21, 1994.
 
ATTACHMENT TO AEP:NRC: 12120 Page 3
A rework condition report was not initiated following the May 17 failure due to an error in the Maintenance Administrative Procedure (MAP) ¹MA3.3-05, "Maintenance Planning".
MAP ¹MA3.3-05 incorrectly defined rework as similar work performed within 30 days of the original failure, rather than 90 days.
As a result of this error the maintenance planner failed to identify the reoccurrence of the packing leak on May 17,
: 1994, as falling within the definition of rework.
3.
Cor ective Actions Taken and esults eyed The work control process code was changed on the 2-MMO-240 repair Job Order.
The 2-MMO-240 repair task now appears on the forced outage
: schedule, as well as within the scope of the refueling outage.
MAP
¹MA3.3-05, "Maintenance Planning,"
was revised to reflect the current definition of rework contained in PMI-7030.
4.
Corrective Actions Taken to Avoid Further Violations PMI-7030, "Corrective Action," will be revised to redefine rework.
The definition for rework will now include any corrective maintenance which requires entry into a Limiting Condition of Operation (LCO) if similar work has been performed on that equipment/component during the current operating cycle, including the previous refueling outage.
When rework of this type occurs, a Condition Report willbe written to aid in the identification/evaluation of an adverse trend.
The "90-day" standard will be retained for work upon equipment or components which do not initiate an LCO entry.
MAP ¹MA3.3-05, "Maintenance Planning," will be revised to refer to PMI-7030 for the above-described redefinition of rework.
These measures will assure that this type of condition will be precluded in the future.
5.
ate When Full Com lienee Will Be Achieved PMI-7030 and MAP modifications will be completed by September 30, 1994.
 
ATTACHMENT TO AEP:NRC:1212G Page 4
The valve stem replacement for 2-MMO-240 will be completed during the first Mode 5 forced outage of sufficient duration or the upcoming Unit 2
refueling
: outage, scheduled to commence September 6, 1994, whichever occurs first.}}

Latest revision as of 14:14, 7 January 2025

Responds to NRC Re Violation Noted in Insp Repts 50-315/94-13 & 50-316/94-13.Corrective Actions:Work Control Process Code Was Changed on 2-MMO-240 Repair Job Order & CAP PMI-7030 Will Be Revised to Redefine Rework
ML17332A260
Person / Time
Site: Cook  American Electric Power icon.png
Issue date: 08/19/1994
From: Fitzpatrick E
INDIANA MICHIGAN POWER CO. (FORMERLY INDIANA & MICHIG
To: Martin J
NRC OFFICE OF INFORMATION RESOURCES MANAGEMENT (IRM)
References
AEP:NRC:1212G, NUDOCS 9408240071
Download: ML17332A260 (10)


Text

(ACCELERATED RIDS PROCESSING)

REGULATORY INFORMATION DISTRIBUTION SYSTEM (RIDS)

'CESSION NBR:9408240071 DOC.DATE: 94/08/19 NOTARIZED: YES DOCKET FACIL:50-315 Donald C.

Cook Nuclear Power Plant, Unit 1, Indiana M

05000315 50-316 Donald C.

Cook Nuclear Power Plant, Unit 2, Indiana M

05000316 AUTH.NAME AUTHOR AFFILIATION FITZPATRICK,E.

Indiana Michigan Power Co.

(formerly Indiana

& Michigan Ele RECIP.NAME RECIPIENT AFFILIATION Document Control Branch (Document Control Desk)

SUBJECT:

Responds to NRC 940720 ltr re violations noted in insp rept 50-315/94-13

& 50-316/94-13.Corrective actions:work control process code was changed on 2-MMO-240 repair job order PMI-7030 will be revised to redefine rework.

DISTRIBUTION CODE:

IE01D COPIES RECEIVED:LTR ENCL SIZE:

TITLE: General (50 Dkt)-Insp Rept/Notice of Vio ation Response NOTES:

RECIPIENT ID CODE/NAME PD3-1 PD INTERNAL: AEOD/DEIB AEOD/S PD/RRAB DEDRO NRR/DRCH/HHFB, NUDOCS-ABSTRACT OGC/HDS2 RES/HFB EXTERNAL EG &G/ BRYCE i J

~ H ~

NRC PDR COPIES LTTR ENCL 1

1 1

1 1

1 1

1 1

1 1

1 1

1 1

1 1

1 1

1 RECIPIENT ID CODE/NAME HICKMAN,J AEOD/SPD/RAB AEOD/TTC NRR/DORS/OEAB NRR/PMAS/IRCB-E 0

R REG FIL 02 GN3 FILE 01 NOAC COPIES LTTR ENCL 1

1 1

1 1

1 1

1 1

1 1

1 1

1 1

1 1

1 NOTE TO ALL"RIDS" RECIPIENTS:

PLEASE HELP US TO REDUCE iVASTE!CONTACTTHE DOCUMENTCONTROL DESK, ROOM Pl-37 (EXT. 504-2083 ) TO ELIMINATEYOUR NAME F ROTI DISTRIBUTIONLISTS FOR DOCUMENTS YOU DON"I'EED!

TOTAL NUMBER OF COPIES REQUIRED'TTR 19 ENCL 19

Indiana Michigan Power Company P.O. Box 16631 Columbus, OH 43216 INDIANA NICHIGAN POWER AEP;NRC'1212G 10 CFR 2.201 Donald C.

Cook Nuclear Plant Units 1 and 2

Docket Nos.

50-315 and 50-316 License Nos.

DPR-58 and DPR-74 NRC INSPECTION REPORTS NO. 50-315/94013 (DRP)

AND 50-316/94013 (DRP)

REPLY TO NOTICE OF VIOLATION U.

S. Nuclear Regulatory Commission Document Control Desk Washington, D.

C.

20555 Attn:

Mr. J.

B. Martin August 19, 1994

Dear Mr. Martin:

This letter is in response to a USNRC letter dated July 20,

1994, that forwarded a notice of violation to Indiana Michigan Power Company.

The notice of violation contained one violation identified during a

routine safety inspection conducted by Messrs. J.

A. Isom, D. J. Hartland, and D. L. Shepard from June 4,

1994, through July 1, 1994.

The violation is associated with the repeated packing failures of a Unit 2 main steam test selector valve over a period of two years that resulted in several entries into four-hour limiting conditions of operation.

Our reply to the notice of violation is provided in the attachment to this letter.

This letter is submitted pursuant to 10 CFR 50.54(f) and, as such, an oath statement is attached.

p~W)

Vice President ar Attachment 940S240071 94081 PDR ADDCI; 05000315PDFi'gy

/

Mr. J.

B. Martin AEP:NRC:1212G CC:

A. A. Blind G. Charnoff W. T. Russell, NRC - Washington, D.C.

NRC Resident Inspector NFEM Section Chief J.

R. Padgett

STATE OF OHIO COUNTY OF FRANKLIN E.

E. Fitzpatrick, being duly sworn, deposes and says that he is the Vice President of licensee Indiana Michigan Power

Company, that he has read the foregoing response to NRC INSPECTION REPORTS NO. 50-315/94013 (DRP)

AND 50-316/94013 (DRP),

REPLY TO NOTICE OF VIOLATION and knows the contents thereof; and that said contents are true to the best of his knowledge and belief.

Subscribed end sworn to before me this ~PE day of 19~EX NOTARY PUBLIC Ale D. HILL gpgpy pUQUC, STAIE pF plllp SSX SSh',IEISSISS EXPIRES~

ATTACHMENT TO AEP:NRC:1212G REPLY TO NOTICE OF VIOLATION

ATTACHMENT TO AEP:NRC:1212G Page

1 Background

A routine safety inspection was conducted by Messrs.

James A. Isom, David J. Hartland, and Douglas L. Shepard from Jurie 4, 1994, through July 1, 1994.

During this inspection, one item was found to be in violation.

The violation was identified as the failure to correct che root cause for the repeated packing failures of a Unit 2 main steam test selector valve over a period of two years that resulted in several entries into four-hour limiting conditions of operation.

This violation was set forth in a letter containing the notice of violation, dated July 20, 1994, fromMr. E.

G. Greenman, Director, Division of Reactor Projects, USNRC, Region III.

The letter was received July 25, 1994.

Our response to the notice of violation is contained within this document.

NRC Violation "10 CFR 50, Appendix B, Criterion XVI, "Corrective Action,"

requires in part that "Measures shall be established to assure that conditions adverse to quality are promptly identified and corrected.

In the case of significant conditions adverse to quality, the measures shall assure that the cause of the condition is determined and corrective action taken to preclude repetition."

Contrary to the

above, as of July 1, 1994, the licensee failed to replace the pitted valve stem on main steam stop valve (MSSV) dump valve test
selector, 2-MM0-240, a

significant condition adverse to quality.

Specifically, Action Request 25594 had been written on July 8,'992, to replace the pitted valve stem but was not scheduled to be performed until the refueling outage starting in September 1994.

Consequently, 2-MMO-240 had to be repacked five times, requiring entries into the four hour Limiting Condition of Operation (LCO),

as required by Technical Specification (TS) 4.7.1.5.1.

There were several opportunities since July 1992 to replace the stem without entering the LCO.

This is a Severity Level IV violation (Supplement I).

ATTACHMENT TO AEP:NRC: 1212G Page 2

Response

to Violation dmissio or Denial o the Alle ed Violat o Indiana Michigan Power Company admits to the violation as cited in the NRC notice of violation.

2.

easons for the Violatio The root cause for this violation has been identified as a

programmatic weakness in the plant's corrective action program.

In July 1992, Unit 2 was in Mode 3 (Hot Standby).

While repacking 2-MM0-240, the valve stem was found to be pitted, scored and in need of replacement.

At that time an Action Request was initiated to replace the stem.

Since a repair activity of this type requires cooldown to Mode 5

to perform, a scheduling code of U2R94 was assigned, adding the repair to the scope of the 1994 refueling outage.

At the time the U2R94 code was assigned, in the absence of prior failure history, this was the correct designation.

The valve stem replacement would only have been elevated to the forced outage schedule if the subsequent, repeated repairs had been identified as rework and an adverse trend.

Since the valve stem deficiency was first identified, 2-MMO-240 has been repacked five additional times.

Had the valve stem replacement been scheduled as a forced outage activity, there would have been two opportunities prior to the violation to complete the repair.

The first opportunity occurred in August 1993 when the unit experienced a reactor trip and forced outage.

The second opportunity occurred in January 1994 when the unit was removed from service to repair an unisolable steam leak on Steam Generator 21 blowdown line.

Repeated packing replacements were not identified in the plant's Corrective Action Program (PMI-7030) as an adverse trend.

PMI-7030, "Corrective Action Program,"

requires a

condition report to be written for similar corrective maintenance work within 90 days of the original deficiency.

Only the final packing failure on May 17, 1994, fell within the 90 day criteria, as this failure occurred 57 days after the previous repair on March 21, 1994.

ATTACHMENT TO AEP:NRC: 12120 Page 3

A rework condition report was not initiated following the May 17 failure due to an error in the Maintenance Administrative Procedure (MAP) ¹MA3.3-05, "Maintenance Planning".

MAP ¹MA3.3-05 incorrectly defined rework as similar work performed within 30 days of the original failure, rather than 90 days.

As a result of this error the maintenance planner failed to identify the reoccurrence of the packing leak on May 17,

1994, as falling within the definition of rework.

3.

Cor ective Actions Taken and esults eyed The work control process code was changed on the 2-MMO-240 repair Job Order.

The 2-MMO-240 repair task now appears on the forced outage

schedule, as well as within the scope of the refueling outage.

MAP

¹MA3.3-05, "Maintenance Planning,"

was revised to reflect the current definition of rework contained in PMI-7030.

4.

Corrective Actions Taken to Avoid Further Violations PMI-7030, "Corrective Action," will be revised to redefine rework.

The definition for rework will now include any corrective maintenance which requires entry into a Limiting Condition of Operation (LCO) if similar work has been performed on that equipment/component during the current operating cycle, including the previous refueling outage.

When rework of this type occurs, a Condition Report willbe written to aid in the identification/evaluation of an adverse trend.

The "90-day" standard will be retained for work upon equipment or components which do not initiate an LCO entry.

MAP ¹MA3.3-05, "Maintenance Planning," will be revised to refer to PMI-7030 for the above-described redefinition of rework.

These measures will assure that this type of condition will be precluded in the future.

5.

ate When Full Com lienee Will Be Achieved PMI-7030 and MAP modifications will be completed by September 30, 1994.

ATTACHMENT TO AEP:NRC:1212G Page 4

The valve stem replacement for 2-MMO-240 will be completed during the first Mode 5 forced outage of sufficient duration or the upcoming Unit 2

refueling

outage, scheduled to commence September 6, 1994, whichever occurs first.