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{{#Wiki_filter:.
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                  *
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                                  U.S. NUCLEAR REGULATORY COMMISSION
U.S. NUCLEAR REGULATORY COMMISSION
                                                  REGIONlli
REGIONlli
                        Docket Nos:         50-266;50-301
Docket Nos:
                        Licenses No:       DPR-24; DPR-27
50-266;50-301
                        Report No:         50-266/98006(DRP); 50-301/98006(DRP)
Licenses No:
                      Licensee:           Wisconsin Electric Power Company
DPR-24; DPR-27
                      Facility:           Point Beach Nuclear Power Plant, Units 1 & 2
Report No:
                      Location:           6612 Nuclear Road
50-266/98006(DRP); 50-301/98006(DRP)
                                          Two Rivers, WI 54241-9516
Licensee:
                      Dates:             fiarch 3 through April 13,1998
Wisconsin Electric Power Company
                      Inspectors:         F. Brown, Senior Resident inspector
Facility:
                                          P. Louden, Resident inspector
Point Beach Nuclear Power Plant, Units 1 & 2
                                          P. Simpson, Resident inspector
Location:
                      Approved by:       J. W. McCormick-Barger, Cliief
6612 Nuclear Road
                                          Reactor Projects Branch 7
Two Rivers, WI 54241-9516
Dates:
fiarch 3 through April 13,1998
Inspectors:
F. Brown, Senior Resident inspector
P. Louden, Resident inspector
P. Simpson, Resident inspector
Approved by:
J. W. McCormick-Barger, Cliief
Reactor Projects Branch 7
9805140331 980505
9805140331 980505
PDR
PDR
G              ADOCK 05000266
ADOCK 05000266
                          PM
G
PM
_ _ - _ _ _ _
_ _ - _ _ _ _


. .
.
      9
.
                                            EXECUTIVE SUMMARY
9
                                    Point Beach Nuclear Plant, Units 1 & 2
EXECUTIVE SUMMARY
                    NRC Inspection Report No. 50-266/98006(DRP); 50-301/98006(DRP)
Point Beach Nuclear Plant, Units 1 & 2
    This inspection includM aspects of licensee operations, engineering, maintenance, and plant
NRC Inspection Report No. 50-266/98006(DRP); 50-301/98006(DRP)
      support. The report covers a six-week inspection period by the resident inspectors.
This inspection includM aspects of licensee operations, engineering, maintenance, and plant
    Operations
support. The report covers a six-week inspection period by the resident inspectors.
    .
Operations
              Operations personnel involved with the restart of the Unit 2 reactor exercised good
Operations personnel involved with the restart of the Unit 2 reactor exercised good
            control of reactivity changes. Clear, consistent communications were used by operators.
.
            (Section 01.1)
control of reactivity changes. Clear, consistent communications were used by operators.
    .      A reactor operator who was "at the controls" for a unit that was shut down and defueled,
(Section 01.1)
            left the authorized surveillance area for a short period of time without being appropriately
A reactor operator who was "at the controls" for a unit that was shut down and defueled,
            relieved by another reactor operator. This action was contrary to the requirements of the
.
            licensee procedure for the conduct of operations and was a violation of Criterion V,
left the authorized surveillance area for a short period of time without being appropriately
            " Instructions, Procedures, and Drawings," of 10 CFR Part 50, Appendix B. (Section 01.2)
relieved by another reactor operator. This action was contrary to the requirements of the
    .
licensee procedure for the conduct of operations and was a violation of Criterion V,
            Operators responded appropriately when the second stage seal of an idle reactor coolant
" Instructions, Procedures, and Drawings," of 10 CFR Part 50, Appendix B. (Section 01.2)
            pump partially opened. Planning of the pump restart and communications and procedure
Operators responded appropriately when the second stage seal of an idle reactor coolant
            adherence during the restart were appropriate and effective. (Section O2.1)
.
    .
pump partially opened. Planning of the pump restart and communications and procedure
            The use of tape to cover the bearing grease port of the residual heat removal pump motor
adherence during the restart were appropriate and effective. (Section O2.1)
            instead of the vendor-designed cover reflected an acceptance of substandard conditions
The use of tape to cover the bearing grease port of the residual heat removal pump motor
            by auxiliary operators. (Section O2.2)
.
    Maintenance
instead of the vendor-designed cover reflected an acceptance of substandard conditions
    .
by auxiliary operators. (Section O2.2)
            Main control board wire separation work was conducted in a professional and thorough
Maintenance
            manner. All work observed was performed with the appropriate work order plan present
Main control board wire separation work was conducted in a professional and thorough
            and in active use. (Section M1.1)
.
    .
manner. All work observed was performed with the appropriate work order plan present
            Maintenance and health physics organizations were not effectively prepared to perform
and in active use. (Section M1.1)
            the lower intemals lift based on planning meetings conducted 24 hours prior to the
Maintenance and health physics organizations were not effectively prepared to perform
            initiation of work. Early in the evolution, maintenance workers failed to follow procedures
.
            resulting in a violation of Technical Specification 15.6.8.1. Laterin the evolution, the
the lower intemals lift based on planning meetings conducted 24 hours prior to the
            maintenance organization displayed better control of the activity, and the lower intemals
initiation of work. Early in the evolution, maintenance workers failed to follow procedures
            were moved without incident. (Section M1.2)
resulting in a violation of Technical Specification 15.6.8.1. Laterin the evolution, the
    .
maintenance organization displayed better control of the activity, and the lower intemals
            Many observed maintenance activities were completed in accordance with requirements
were moved without incident. (Section M1.2)
            specified in administrative and work control procedures. However, ceases were noted
Many observed maintenance activities were completed in accordance with requirements
            where administrative requirements were not being implemented. Some of the corrective
.
            actions for these issues were narrowly focused, and the effort to address the
specified in administrative and work control procedures. However, ceases were noted
            inconsistencies in application of administrative requirements within the maintenance
where administrative requirements were not being implemented. Some of the corrective
            department was not an integrated effort. (Section M1.3)
actions for these issues were narrowly focused, and the effort to address the
                                                        2
inconsistencies in application of administrative requirements within the maintenance
department was not an integrated effort. (Section M1.3)
2


    _ - - _ - _-_ - __-_ _ _ - __ - _- -- _ _- .                                                     .     - _ _ _                                 .
_ - - _ - _-_ - __-_ _ _ - __ - _- -- _ _- .
                                      .
.
  .
- _ _ _
                                                                                                                                                      j
.
                                                        .                                                                                             f
j
                                                .      Maintenance and operations department freeze seal pre-evolution briefings held on
.
                                                        March 17,1998, were thorough and covered command and control responsibilities,
.
                                                      expected communication standards, and contingencies. Teamwork between different
f
                                                      disciplines was evident and participants displayed a good questioning attitude.
.
                                                      (Section M1.5)
Maintenance and operations department freeze seal pre-evolution briefings held on
                                                Enaineerina
.
                                                .    A ventilation control panel in an emergency diesel generator room was misclassified as
March 17,1998, were thorough and covered command and control responsibilities,
                                                      nonsafety-related. The licensee's initial corrective actions did not include determining if
expected communication standards, and contingencies. Teamwork between different
                                                      operability of the system had been challenged while the component was incorrectly
disciplines was evident and participants displayed a good questioning attitude.
                                                      classified as being nonsafety-related. (Section E1.1)
(Section M1.5)
l                                               .
Enaineerina
                                                      The licensee identified and corrected two cases where valves between seismically
A ventilation control panel in an emergency diesel generator room was misclassified as
l                                                     qualified piping systems and non-qualified piping systems were not maintained in a
.
I                                                     closed position as required by the Final Safety Analysis Report. (Section E1.2)
nonsafety-related. The licensee's initial corrective actions did not include determining if
operability of the system had been challenged while the component was incorrectly
classified as being nonsafety-related. (Section E1.1)
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The licensee identified and corrected two cases where valves between seismically
.
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qualified piping systems and non-qualified piping systems were not maintained in a
I
closed position as required by the Final Safety Analysis Report. (Section E1.2)
!
!
                                                .    Offsite, corporate office-based engineering personnel working on a corrective action
Offsite, corporate office-based engineering personnel working on a corrective action
                                                      commitment initiative to assess the adequacy of a separation of seismically qualified and
.
!                                                     non-qualified piping systems were performing analyses and taking credit for components
commitment initiative to assess the adequacy of a separation of seismically qualified and
                                                      to function in a manner that may not have previously been considered in the design basis.
!
                                                      The engineers had not evaluated whether such reliance might constitute a design basis
non-qualified piping systems were performing analyses and taking credit for components
j                                                     change. Additionally, onsite licensee personnel performing concurrent and interrelated
to function in a manner that may not have previously been considered in the design basis.
;                                                     corrective action initiatives had not been informed of the potential design engineering
The engineers had not evaluated whether such reliance might constitute a design basis
                                                      activities that could have affected the results of these other initiatives. (Section E1.3)
j
                                                .    The inspectors concluded that the 125-Volt direct current (Vde) system was capable of
change. Additionally, onsite licensee personnel performing concurrent and interrelated
l                                                     meeting design basis functions. However, the failure to maintain an up-to-date battery
;
                                                      loading calculation was considered a violation of 10 CFR Part 50, Appendix B,
corrective action initiatives had not been informed of the potential design engineering
                                                      Criterion Ill, " Design Control." (Section E3.1)
activities that could have affected the results of these other initiatives. (Section E1.3)
                                                                                                                                                      l
The inspectors concluded that the 125-Volt direct current (Vde) system was capable of
                                                .    The reactor engineering organization did not provide accurate critical rats position data to
.
l
meeting design basis functions. However, the failure to maintain an up-to-date battery
loading calculation was considered a violation of 10 CFR Part 50, Appendix B,
Criterion Ill, " Design Control." (Section E3.1)
The reactor engineering organization did not provide accurate critical rats position data to
.
l
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operations personnel during an initial attempt to startup Unit 2. The problems revealed
'
'
                                                      operations personnel during an initial attempt to startup Unit 2. The problems revealed
during the startup were considered additional examples of reactor engineering
                                                      during the startup were considered additional examples of reactor engineering
performance concems which were the subject of a Notice of Violation from Inspection
                                                      performance concems which were the subject of a Notice of Violation from Inspection
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l                                                     Report No. 50-266/98003(DRP); 50-301/98003(DRP). (Section E3.2)
Report No. 50-266/98003(DRP); 50-301/98003(DRP). (Section E3.2)
l
The practice of duty technical advisors (DTAs) serving two consecutive 24-hour watches
.
was not consistent with the intent of program procedures and raised questions regarding
the DTA's fitness-for-duty. Although, no specific performance issues were identified as a
result of the DTA standing consecutive watches, licensee management immediately
revised expectations regarding this practice to preclude potential fitness-for-duty issues.
(Section E6.1)
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                                                .    The practice of duty technical advisors (DTAs) serving two consecutive 24-hour watches
1
                                                      was not consistent with the intent of program procedures and raised questions regarding
I
                                                      the DTA's fitness-for-duty. Although, no specific performance issues were identified as a
I
                                                      result of the DTA standing consecutive watches, licensee management immediately
l
                                                      revised expectations regarding this practice to preclude potential fitness-for-duty issues.
3
                                                      (Section E6.1)
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                                                                                                                                                      1
I                                                                                                                                                     I
                                                                                                                                                      l
                                                                                                                                                      l
                                                                                                  3
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L_________-------__---__---._---------__
L_________-------__---__---._---------__


, - _ _ _ - _ _ - _ _ _ _ _ - _ _ - - _ _ - _ _ _ _ - - - _ _ _                 -
, - _ _ _ - _ _ - _ _ _ _ _ - _ _ - - _ _ - _ _ _
                .
_ - -
                      .
-
                      Plant Support
_ _ _
                      .          Perronnel exposures during the Unit i refueling outage were meeting established
-
  .
.
                                  licensee goals. The number of personnel contamination events was higher than
.
l                                 anticipated; however, most of the events were minor shoe contaminations. The health
Plant Support
                                  physics manager initiated a review of the causes for the higher than anticipated number
Perronnel exposures during the Unit i refueling outage were meeting established
                                  of personnel contamination events. None of the events resulted in significant exposure of
.
!                                 personnel. (Section R1.1)
.
                                                                                                                            l
licensee goals. The number of personnel contamination events was higher than
                                                                                                                            I
l
                                                                                                                            1
anticipated; however, most of the events were minor shoe contaminations. The health
                                                                                                                            l
physics manager initiated a review of the causes for the higher than anticipated number
                                                                                                                            l
of personnel contamination events. None of the events resulted in significant exposure of
                                                                                                                            '
!
personnel. (Section R1.1)
l
I
1
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'
l
l
f
f
I
I
l
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i                                                                         4                                                 I
i
!                                                                                                                           1
4
                                                                                                              _ _ _ . _
I
!
1
_ _ _ . _


  ._ _ _ _ _ _ _ _ _ _ _ _ _ _ - _ _ _ _ _ _ _ _ _ - - -                                       ._ _       . _ _ _ _                     _               .
._ _ _ _ _ _ _ _ _ _ _ _ _ _ - _ _ _ _ _ _ _ _ _ - - -
              .                       .
._ _
                                                              *
. _ _ _ _
                                                      .
_
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*
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                                                                                                    Report Details
Report Details
                                                    Summary of Plant Status
Summary of Plant Status
                                                    During this inspection period, Unit 1 was shutdown in a continuation of the Cycle 24 refueling
During this inspection period, Unit 1 was shutdown in a continuation of the Cycle 24 refueling
                                                    outage. ' Unit 2 was shutdown on March 5,1998, in accordance with Technical Specification
outage. ' Unit 2 was shutdown on March 5,1998, in accordance with Technical Specification
                                                    (T/S) 15.3.0., because the compenent cooling water (CCW) system was declared inoperable.
(T/S) 15.3.0., because the compenent cooling water (CCW) system was declared inoperable.
                                                    Detailed engineering analysis subsequently determined that the CCW system was operable.-
Detailed engineering analysis subsequently determined that the CCW system was operable.-
                                                    Unit 2 was restarted on March 28,1998, and operated at 100 percent power for the remainder of
Unit 2 was restarted on March 28,1998, and operated at 100 percent power for the remainder of
                                                    the inspection period.
the inspection period.
                                                    Inspection Focus
Inspection Focus
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During this inspection period, the inspectors focused on conduct of plant operations, continued a
vertical slice review of the 125-volt direct current (Vde) system, and completed routine inspection
activities.
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1. Operations
01
Conduct of Operations
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j                                                    During this inspection period, the inspectors focused on conduct of plant operations, continued a
01.1
                                                    vertical slice review of the 125-volt direct current (Vde) system, and completed routine inspection
Unit 2 Reactor Startuo (Inspection Procedure (IP) 71707)
                                                    activities.
During the restart of the Unit 2 reactor on March 28,1998, problems encountered during
the attempt to make the reactor critical resulted in the licensee suspending the criticality
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                                                                                                    1. Operations
attempt. The reactor was made critical later the same day following a review of the
                                                    01      Conduct of Operations
earlier problems and a recalculation of the estimated critical rate position. Problems
l                                                    01.1    Unit 2 Reactor Startuo (Inspection Procedure (IP) 71707)
associated with the initial estimated critical rate position calculation are discussed in
                                                              During the restart of the Unit 2 reactor on March 28,1998, problems encountered during
Section E3.2 of this report. Operations personnelinvolved with the restart of the Unit 2
                                                              the attempt to make the reactor critical resulted in the licensee suspending the criticality
reactor exercised good command and control of reactivity changes and used clear,
l                                                            attempt. The reactor was made critical later the same day following a review of the
consistent three-way communications.
                                                              earlier problems and a recalculation of the estimated critical rate position. Problems
01.2 Unit Operator Left the Authorized "At the Controls" Area
                                                              associated with the initial estimated critical rate position calculation are discussed in
a.
                                                              Section E3.2 of this report. Operations personnelinvolved with the restart of the Unit 2
Inspection Scope (IP 71707)
                                                              reactor exercised good command and control of reactivity changes and used clear,
The inspectors reviewed the circumstances regarding the failure of an onshift reactor
                                                              consistent three-way communications.
operator (control operator (CO)) to remain within authorized surveillance areas in the
                                                    01.2 Unit Operator Left the Authorized "At the Controls" Area
control room.
                                                      a.     Inspection Scope (IP 71707)
;
                                                              The inspectors reviewed the circumstances regarding the failure of an onshift reactor
                                                              operator (control operator (CO)) to remain within authorized surveillance areas in the
;                                                            control room.
l
l
l                                                     b.     Observations and Findingg
l
b.
Observations and Findingg
'
'
                                                                                                                                                            ,
,
                                                              The inspectors were in the control room monitoring a Unit 2 non-routine activity on           ;
The inspectors were in the control room monitoring a Unit 2 non-routine activity on
                                                                                                                                                            I
;
                                                              March 14,1998. At approximately 9:00 p.m., the inspectors noted that the Unit 1 CO was
March 14,1998. At approximately 9:00 p.m., the inspectors noted that the Unit 1 CO was
l                                                             not in an authorized surveillance area for Unit 1, which was defueled at the time. Shortly
l
i.                                                           thereafter, the Unit 1 CO reentered the authorized surveillance area from the control room
not in an authorized surveillance area for Unit 1, which was defueled at the time. Shortly
                                                              back panel area. The CO was absent from the authorized area for about one minute.
i.
                                                              The T/S minimem manning requirements were satisfied during the CO's absence;                   i
thereafter, the Unit 1 CO reentered the authorized surveillance area from the control room
                                                              however, Operations Manual (OM) 1.1, " Conduct of Plant Operations," Revision 1,
back panel area. The CO was absent from the authorized area for about one minute.
                                                                                                          5
The T/S minimem manning requirements were satisfied during the CO's absence;
i
however, Operations Manual (OM) 1.1, " Conduct of Plant Operations," Revision 1,
5
,-
,-
    .
.
!
!


                                              - - - _ _ _ _ - _ - _ _ __- - _ - --__-_ _ .
- - - _ _ _ _ - _ - _ _ __- - _ - --__-_ _ .
.   .
.
                                                                  -
.
                                        .
-
                                                                    Attachment 2, Paragraph 2.3, required the reactor operator "at the controls" to remain in
.
                                                                    the authorized area unless relieved. The inspectors discussed the CO's absence from
Attachment 2, Paragraph 2.3, required the reactor operator "at the controls" to remain in
                                                                    the authorized area with the duty operating supervisor (DOS, a senior reactor operator).
the authorized area unless relieved. The inspectors discussed the CO's absence from
                                                                    The DOS stated that the CO had been released from the authorized area for a short
the authorized area with the duty operating supervisor (DOS, a senior reactor operator).
                                                                    period of time, and that this was acceptable because Unit 1 was defueled. The
The DOS stated that the CO had been released from the authorized area for a short
                                                                    inspectors pointed out that OM1.1 allowed no exceptions. This issue was further
period of time, and that this was acceptable because Unit 1 was defueled. The
                                                                    discussed with the operations manager, who acknowledged that OM 1.1 required the unit
inspectors pointed out that OM1.1 allowed no exceptions. This issue was further
                                                                    CO to remain in the authorized area under all fuel loading conditions. The failure of the
discussed with the operations manager, who acknowledged that OM 1.1 required the unit
                                                                    Unit 1 CO to remain in the authorized area was a violation (VIO 50-266/98006-01(DRP))
CO to remain in the authorized area under all fuel loading conditions. The failure of the
                                                                    of 10 CFR Part 50, Appendix B, Criterion V, " Instructions, Procedures, and Drawings,"
Unit 1 CO to remain in the authorized area was a violation (VIO 50-266/98006-01(DRP))
                                                                    which requires that activities affecting quality be performed in accordance with
of 10 CFR Part 50, Appendix B, Criterion V, " Instructions, Procedures, and Drawings,"
                                                                    procedures. Condition Report (CR) 98-1075 was written to document this event, and the
which requires that activities affecting quality be performed in accordance with
                                                                    operations manager sent all operators an electronic memorandum which reiterated the
procedures. Condition Report (CR) 98-1075 was written to document this event, and the
                                                                    requirements of OM 1.1 for an operator "at the controls."
operations manager sent all operators an electronic memorandum which reiterated the
                                                                    The inspectors also identified a discrepancy in OM 1.1. Figure 1 and Section 2.8 of
requirements of OM 1.1 for an operator "at the controls."
                                                                    Attachment 1 differed concoming the control room area the DOS was to occupy. The
The inspectors also identified a discrepancy in OM 1.1. Figure 1 and Section 2.8 of
                                                                    licensee's practice was to allow the DOS to sit on a raised platform in the control room,
Attachment 1 differed concoming the control room area the DOS was to occupy. The
                                                                    which was consistent with Section 2.8 but was not allowed by Figure 1. The inspectors
licensee's practice was to allow the DOS to sit on a raised platform in the control room,
                                                                    identified the discrepancy to the duty shift superintendent (DSS, a senior reactor
which was consistent with Section 2.8 but was not allowed by Figure 1. The inspectors
                                                                    operator). The DSS stated the discrepancy had already been identified by operations
identified the discrepancy to the duty shift superintendent (DSS, a senior reactor
                                                                    personnel via the procedure change process about six months earlier but was not yet
operator). The DSS stated the discrepancy had already been identified by operations
                                                                    corrected. The DSS wrote a CR to document the discrepancy on March 19,1998. This
personnel via the procedure change process about six months earlier but was not yet
                                                                    discrepancy was corrected the same day with a temporary procedure change.
corrected. The DSS wrote a CR to document the discrepancy on March 19,1998. This
                                                                    During this inspection period, the inspectors noted that the operations department had a
discrepancy was corrected the same day with a temporary procedure change.
                                                                    significant number of outstanding procedure change requests and was in the process of
During this inspection period, the inspectors noted that the operations department had a
                                                                    upgrading operations procedures. Licensee management indicated that priorities were
significant number of outstanding procedure change requests and was in the process of
                                                                    set to accomplish the procedure upgrade work within existing resource constraints. The
upgrading operations procedures. Licensee management indicated that priorities were
                                                                    correction of OM 1.1, identified six months earlier by operators, was not high in the
set to accomplish the procedure upgrade work within existing resource constraints. The
                                                                    priority scheme. The inspectors commented to operations management that procedural
correction of OM 1.1, identified six months earlier by operators, was not high in the
                                                                    adherence and operator identification of needed procedure changes may be adversely
priority scheme. The inspectors commented to operations management that procedural
                                                                    affected given the large backlog which impacted the timeliness of processing procedure
adherence and operator identification of needed procedure changes may be adversely
                                                                    changes. However, the inspectors noted that progress was being made in upgrading
affected given the large backlog which impacted the timeliness of processing procedure
                                                                    operations department procedures overall.
changes. However, the inspectors noted that progress was being made in upgrading
                                            c.                       Conclusions
operations department procedures overall.
                                                                    The inspectors concluded that the CO who left the "at the controls" area for a bnef time
c.
                                                                    on March 14,1998, without obtaining an appropriate relief, was not performing duties in
Conclusions
                                                                    accordance with OM 1.1. This was considered a violation of 10 CFR Part 50,
The inspectors concluded that the CO who left the "at the controls" area for a bnef time
                                                                    Appendix B. The inspectors also identified a discrepancy in OM 1.1, which the licensee
on March 14,1998, without obtaining an appropriate relief, was not performing duties in
                                                                    subsequently corrected. The procedure upgrade program contained a substantial
accordance with OM 1.1. This was considered a violation of 10 CFR Part 50,
                                                                    backlog of identified changes that needed to be made; however, a prioritization list was
Appendix B. The inspectors also identified a discrepancy in OM 1.1, which the licensee
                                                                    being followed and some progress was being made.
subsequently corrected. The procedure upgrade program contained a substantial
                                                                                                              6
backlog of identified changes that needed to be made; however, a prioritization list was
  _ _ _ _ _ _ _ _ _ _ _ _ _ _ - - - . _ _ _                                                 _                                                                 I
being followed and some progress was being made.
6
_ _ _ _ _ _ _ _ _ _ _ _ _ _ - - - . _ _ _
_
I


--                                   _ _ _ - - _ _ - - ___ - _-                                         ___ ___ -__-- _ _
--
        .                 .
_ _ _ - - _ _ - - ___ - _-
                                                                -
___ ___ -__-- _ _
                                        .
.
                                      02                         Operational Status of Facilities and Equipment
.
                                      O2.1                       Reactor Coolant Pumo (RCP) Seal Leakaae
-
                                              a.                 (nspection Scope (IP 71707)
.
                                                                The inspectors reviewed the licensee's response to excessive leakage from the
02
                                                                Unit 2 "B" RCP (2P-1B) second stage seal.
Operational Status of Facilities and Equipment
                                              b.                 Observations and Findings
O2.1
                                                                On March 10,1998, operators noted excessive flow through the second stage seal of
Reactor Coolant Pumo (RCP) Seal Leakaae
                                                                RCP 2P-1B. Unit 2 was in cold shutdown and reactor coolant pressure was 300 pounds
a.
                                                                per square inch gauge (psig) with the "A" RCP (2P-1 A) operating and the "B" RCP (2P-
(nspection Scope (IP 71707)
                                                                  1B) idle. Upon the discovery of the excessive seal leakage, the operating crew entered   ;
The inspectors reviewed the licensee's response to excessive leakage from the
                                                                Abnormal Operating Procedure 18. "RCP Malfunction," Revision 8. In accordance with         i
Unit 2 "B" RCP (2P-1B) second stage seal.
                                                                that procedure, pump 2P-1 A was secured, the reactor was depressurized to about           i
b.
                                                                50 psig, and tne RCP seal water retum valves were closed. These actions terminated         ,
Observations and Findings
                                                                the excessive flow. The inspectors noted thet the operating crew referenced the           j
On March 10,1998, operators noted excessive flow through the second stage seal of
                                                                appropriate T/S for reactor coolant system leakage. The licensee wrote a condition report I
RCP 2P-1B. Unit 2 was in cold shutdown and reactor coolant pressure was 300 pounds
                                                                to document the event.                                                                   l
per square inch gauge (psig) with the "A" RCP (2P-1 A) operating and the "B" RCP (2P-
                                                                The licensee formed a multi-disciplinary team to assess the condition of the 2P-1B seal
1B) idle. Upon the discovery of the excessive seal leakage, the operating crew entered
                                                                package and concluded that the second stage seal had partially opened, but had not
;
                                                                failed. A temporary change was made to Operating Procedure (OP) 3C, " Hot Shutdown       1
Abnormal Operating Procedure 18. "RCP Malfunction," Revision 8. In accordance with
                                                                to Cold Shutdown," Revision 69, to provide instructions for starting 2P-1B to allow for
i
                                                                further evaluation of the seal's condition. The inspectors reviewed the change to OP 3C
that procedure, pump 2P-1 A was secured, the reactor was depressurized to about
                                                                and the referenced sections of OP 4B, "RCP Operation," Revision 34, and concluded that
i
                                                                the changes were appropriate for the circumstances. An operating crew started
50 psig, and tne RCP seal water retum valves were closed. These actions terminated
                                                                  RCP 2P-1B without incident on March 14,1998. The second stage seal reseated during
,
                                                                the pump start. The inspectors observed appropriate and effective communications,
the excessive flow. The inspectors noted thet the operating crew referenced the
                                                                planning, and performance of pump start activities in the control room during this
j
                                                                evolution.
appropriate T/S for reactor coolant system leakage. The licensee wrote a condition report
                                              c.               Conclusions
I
                                                                Operators responded appropriately when the second stage seal of an idle RCP partially
to document the event.
l                                                               opened. Planning of the pump restart and communications and procedure adherence
l
                                                                during the restart were appropriate and effective.
The licensee formed a multi-disciplinary team to assess the condition of the 2P-1B seal
                                      O2.2 Residual Heat Removal (RHR) Pump Motor Grease (IP 71707)
package and concluded that the second stage seal had partially opened, but had not
                                                                                                                                                            i
failed. A temporary change was made to Operating Procedure (OP) 3C, " Hot Shutdown
                                                                  During a routine walkdown of safety-related systems, the inspectors identified a           ,
1
                                                                  discrepancy in the amount of grease present on the outboard bearings of the               l
to Cold Shutdown," Revision 69, to provide instructions for starting 2P-1B to allow for
l                                                               four RHR pump motors. The amount ranged from grease fully covering the bearings to
further evaluation of the seal's condition. The inspectors reviewed the change to OP 3C
                                                                  being hardly visible. The inspectors also noted that tape was used to cover the
and the referenced sections of OP 4B, "RCP Operation," Revision 34, and concluded that
                                                                  Unit 1 RHR "A" pump motor outboard bearing grease port in lieu of the vendor-designed   i
the changes were appropriate for the circumstances. An operating crew started
                                                                cover. When notified of the findings, the component engineers investigated the situation
RCP 2P-1B without incident on March 14,1998. The second stage seal reseated during
                                                                  and informally determined that the pumps were still operable. Operations personnel
the pump start. The inspectors observed appropriate and effective communications,
                                                                                                                          7
planning, and performance of pump start activities in the control room during this
- _ _ _ _ _ _ _ _ _ _ _ - _ _ _ _ _ _ - _ - _ _ - - - - _ _ _ - -
evolution.
c.
Conclusions
Operators responded appropriately when the second stage seal of an idle RCP partially
l
opened. Planning of the pump restart and communications and procedure adherence
during the restart were appropriate and effective.
O2.2 Residual Heat Removal (RHR) Pump Motor Grease (IP 71707)
i
During a routine walkdown of safety-related systems, the inspectors identified a
,
discrepancy in the amount of grease present on the outboard bearings of the
l
l
four RHR pump motors. The amount ranged from grease fully covering the bearings to
being hardly visible. The inspectors also noted that tape was used to cover the
Unit 1 RHR "A" pump motor outboard bearing grease port in lieu of the vendor-designed
i
cover. When notified of the findings, the component engineers investigated the situation
and informally determined that the pumps were still operable. Operations personnel
7
- _ _ _ _ _ _ _ _ _ _ _ - _ _ _ _ _ _ - _ - _ _ - - - - _ _ _ - -


    _ _ _ - _ _ _ _ _ - _ _ _ - - _ _ _ _ _ _ _ _ _ _ - _ _ _ _ _ _ _ _ _ _ _ _ _ _ - _ _ _ _ _ _ _ , _ -                                                                 ____ __ ___       _   _ _ _ _ _
_ _ _ - _ _ _ _ _ - _ _ _ - - _ _ _ _ _ _ _ _ _ _ - _ _ _ _ _ _ _ _ _ _ _ _ _ _ - _ _ _ _ _ _ _ , _ -
  .                             .
____ __ ___
                                                                                                                                                                                                            1
_
                                                          .
_ _ _ _ _
                                                                                                    -
1
                                                                                                                                                                                                            J
.
                                                                                                                                                                                                            :
.
                                                                                                                                                                                                            l
J
                                                                                                                                                                                                            l
-
                                                                                                        wrote a condition report regarding the matter and requested a formal operability                   I
.
                                                                                                        determination (OD). The licensee concluded in the OD that the pumps remained
:
                                                                                                        operable.
l
1                                                                                                                                                                                                           1
l
                                                                                                        The inspectors concluded that the bearing grease levels were not an operability concem.
wrote a condition report regarding the matter and requested a formal operability
I
determination (OD). The licensee concluded in the OD that the pumps remained
operable.
1
1
'
'
                                                                                                                                                                                                            l
The inspectors concluded that the bearing grease levels were not an operability concem.
L                                                                                                         However, the use of tape to cover the bearing grease port of the safety-related
l
                                                                                                        RHR pump instead of the vendor-designed cover reflected auxiliary operator acceptance
L
                                                                                                        of substandard conditions.
However, the use of tape to cover the bearing grease port of the safety-related
                                                          O3                                           Operations Procedures and Documentation                                                           ;
RHR pump instead of the vendor-designed cover reflected auxiliary operator acceptance
                                                          O3.1                                           Update on Station Wide Procedure Uparade Proaram (IPs 71707. 62707. and 37551)
of substandard conditions.
                                                                                                        In a previous inspection report (No. 50-266/97020(DRP); 50-301/97020(DRP)), the
O3
                                                                                                        inspectors opened an inspection follow up item (IFI) to evaluate the licensee's ongoing
Operations Procedures and Documentation
                                                                                                        procedure upgrade program and verify that:                                                         j
;
                                                                                                        .        upper tier administrative procedures for procedure adherence and procedural
O3.1
                                                                                                                control of activities were consistent wia the current licensing basis and NRC
Update on Station Wide Procedure Uparade Proaram (IPs 71707. 62707. and 37551)
                                                                                                                guidance,
In a previous inspection report (No. 50-266/97020(DRP); 50-301/97020(DRP)), the
i                                                                                                                                                                                                           q
inspectors opened an inspection follow up item (IFI) to evaluate the licensee's ongoing
procedure upgrade program and verify that:
j
upper tier administrative procedures for procedure adherence and procedural
.
control of activities were consistent wia the current licensing basis and NRC
guidance,
i
q
l
l
                                                                                                        *        the methods for establishing procedural controis were commensurate with                   J
the methods for establishing procedural controis were commensurate with
L                                                                                                               licensee staff training and supervisory oversight such that activities affecting           i
J
                                                                                                                safety were performed in a controlled manner and with predictable results, and
*
                                                                                                        +        the licensee's process for assuring that work plans were not inappropriately used
L
                                                                                                                to circumvent procedural change requirements were adequate.                               ]
licensee staff training and supervisory oversight such that activities affecting
                                                                                                                                                                                                            I
i
                                                                                                        Over the past six months, the inspectors have identified several instances where
safety were performed in a controlled manner and with predictable results, and
                                                                                                        procedural controls were either inadequate for the circumstances or were not adhered to             l
the licensee's process for assuring that work plans were not inappropriately used
                                                                                                        by licensee personnel. Sections 01.2, M1.2, M1.3, and E3.2 of this report discuss other             i
+
                                                                                                        examples of procedural problems still evident at the station.                                       .
to circumvent procedural change requirements were adequate.
                                                                                                                                                                                                            I
]
                                                                                                        Notwithstanding these problems, the inspectors have noted an increased sensitivity to
I
                                                                                                        procedural quality issues and some progress in upgrading procedures. Additionally,
Over the past six months, the inspectors have identified several instances where
                                                                                                        insufficient time has passed to determine the effect of the licensee' procedure upgrade
procedural controls were either inadequate for the circumstances or were not adhered to
                                                                                                        project. Therefore, the inspectors will leave IFl 50-266/97020-02(DRP);
l
                                                                                                        50-301/97020-02(DRP) open for an additional six-month period to track the programmatic
by licensee personnel. Sections 01.2, M1.2, M1.3, and E3.2 of this report discuss other
                                                                                                        aspects of procedure content, use, and adherence.
i
                                                        07                                             Quality Assurance in Operations
examples of procedural problems still evident at the station.
                                                        07.1 Operations Quality Assurance Audii(IP 71707)
.
                                                                                                      The inspectors attended a quality assurance department audit exit on March 13,1998.
I
                                                                                                      The audit focused on operations department administrative controls and operator                     4
Notwithstanding these problems, the inspectors have noted an increased sensitivity to
                                                                                                        performance. The meeting was well attended by operations department personnel and
procedural quality issues and some progress in upgrading procedures. Additionally,
                                                                                                        plant management. Operations management was receptive to the auditors' findings. The
insufficient time has passed to determine the effect of the licensee' procedure upgrade
                                                                                                        inspectors noted that most of the findings from the audit were more administrative in
project. Therefore, the inspectors will leave IFl 50-266/97020-02(DRP);
                                                                                                      nature rather than performance-based. The inspectors subsequently reviewed the issued
50-301/97020-02(DRP) open for an additional six-month period to track the programmatic
                                                                                                                                                    8
aspects of procedure content, use, and adherence.
-                                                       _ _ _ _ - _ _ _ _ _ - _ -
07
Quality Assurance in Operations
07.1 Operations Quality Assurance Audii(IP 71707)
The inspectors attended a quality assurance department audit exit on March 13,1998.
The audit focused on operations department administrative controls and operator
4
performance. The meeting was well attended by operations department personnel and
plant management. Operations management was receptive to the auditors' findings. The
inspectors noted that most of the findings from the audit were more administrative in
nature rather than performance-based. The inspectors subsequently reviewed the issued
8
-
_ _ _ _ - _ _ _ _ _ - _ -


                                      __ -____-_______________ _ -___-_ ______ _ __-_____ _ - _ _ _
__ -____-_______________ _ -___-_ ______ _ __-_____ _ - _ _ _
  . ,                                                                                                                   l
l
            .
.
            audit report (No. A-P-98-03) and verified that the issues discussed at the exit meeting
,
            were consistent with those documented in the report.
.
                                                                                                                      1
audit report (No. A-P-98-03) and verified that the issues discussed at the exit meeting
      08     Miscellaneous Operations issues
were consistent with those documented in the report.
      08.1   (Closed) Licensee Event Report (LER) 50-266/98004: 50-301/98004: Resc.or coolant
1
            pump lube oil collection system design nonconformance with Appendix R, Section 111.0.                     1
08
                                                                                                                      '
Miscellaneous Operations issues
            This issue was discussed and dispositioned in accordance with the NRC Enforcement
08.1
            Policy in inspection Report No. 50-266/98003(DRP); 50-301/98003(DRP), Section O2.1.
(Closed) Licensee Event Report (LER) 50-266/98004: 50-301/98004: Resc.or coolant
            No further action is necessary regarding this matter.
pump lube oil collection system design nonconformance with Appendix R, Section 111.0.
      08.2 (Closed) LER 50-301/98002: Reactor coolant pump component cooling water retum line                           I
1'
            check valve found seriously degraded. The CCW system containment retum check
This issue was discussed and dispositioned in accordance with the NRC Enforcement
            valve (2CC-745) was radiographer and found in the open position. This valve provides a
Policy in inspection Report No. 50-266/98003(DRP); 50-301/98003(DRP), Section O2.1.
            redundant means for preventing loss of CCW fluid in the event of a failure of a CCW pipe                   j
No further action is necessary regarding this matter.
08.2 (Closed) LER 50-301/98002: Reactor coolant pump component cooling water retum line
I
check valve found seriously degraded. The CCW system containment retum check
valve (2CC-745) was radiographer and found in the open position. This valve provides a
redundant means for preventing loss of CCW fluid in the event of a failure of a CCW pipe
j
inside the containment. The licensee rebuilt the intamals of the valve and the repairs
!
i
i
            inside the containment. The licensee rebuilt the intamals of the valve and the repairs                    !
were deemed to be adequate. The inspectors had no further questions regarding this
I
'
'
            were deemed to be adequate. The inspectors had no further questions regarding this                        I
matter.
            matter.                                                                                                  I
I
                                                                                                                      I
I
                                                                                                                        !
!
                                                                                                                      l
l
                                                                                                    II. Mainte_n_ance
II. Mainte_n_ance
      M1     Conduct of Maintenance
M1
      M1.1 Main Control Board Wire Separation Maintenance Activities
Conduct of Maintenance
      a.    [nLspection
M1.1 Main Control Board Wire Separation Maintenance Activities
              r          Scope (IP 62707)
[nLspection Scope (IP 62707)
            The inspectors observed and reviewed the following maintenance activities which were
a.
            part of the corrective actions to resolve discrepancies between redundant safety-relsted
r
            equipment:
The inspectors observed and reviewed the following maintenance activities which were
              .      Work Order Plan 9705320, " Sleeve / Wrap Cables For Circuit 1 A-06 Bus                           l
part of the corrective actions to resolve discrepancies between redundant safety-relsted
                      Voltmeter," and
equipment:
            .        Work Order Plan 9705324, " Sleeve / Wrap Cables For Circuit Supply
Work Order Plan 9705320, " Sleeve / Wrap Cables For Circuit 1 A-06 Bus
                      Breaker 1 A52-77 to Bus 1 A-04."
l
            The planned activities included separating and sleeving electrical wires in some control
.
            room panels associated with control and indication circuits for the Class 1E electrical
Voltmeter," and
            buses and power sources,
Work Order Plan 9705324, " Sleeve / Wrap Cables For Circuit Supply
      b.     Observations and Findinos
.
            The scope of the planned cable separation work required entry into the T/S 15.3.7.B.1.g.
Breaker 1 A52-77 to Bus 1 A-04."
            limiting condition for operation (LCO) for Unit 2 (Unit 1 was defueled at the time) since the
The planned activities included separating and sleeving electrical wires in some control
            ' B" train of the 4.16-kilovolt bus safeguards switchgear (Bus 1 A-06) did not have its
room panels associated with control and indication circuits for the Class 1E electrical
            emergency power source available because of the protective tagout boundary. The
buses and power sources,
            inspectors verified that the appropriate T/S LCOs had been entered for the plant
b.
            conditions and scope of planued work.
Observations and Findinos
I                                                                                                             9
The scope of the planned cable separation work required entry into the T/S 15.3.7.B.1.g.
limiting condition for operation (LCO) for Unit 2 (Unit 1 was defueled at the time) since the
' B" train of the 4.16-kilovolt bus safeguards switchgear (Bus 1 A-06) did not have its
emergency power source available because of the protective tagout boundary. The
inspectors verified that the appropriate T/S LCOs had been entered for the plant
conditions and scope of planued work.
I
9


    _ _ _ _ _ _ _         _ _ _       __   _ _ _ _ _             _ _ _ _ _         -- - _ - _ - _ -       _________
_ _ _ _ _ _ _
                                                                                                                            ,
_ _ _
  .               .
__
                                '
_ _ _ _ _
                    .
_ _ _ _ _
                                  The inspectors noted good coordination and communication between the work control
-- - _ - _ - _ -
                                  center, control room, and maintenance personnel. The job supervisor briefed the control
_________
                                  room personnel on the specifics of each work order plan and walked through each
,
                                  package with the maintenance crew doing the work. Quality control personnel were
.
l                                 present whenever required by the work order plans and quality control hold points were
.
'
.
The inspectors noted good coordination and communication between the work control
center, control room, and maintenance personnel. The job supervisor briefed the control
room personnel on the specifics of each work order plan and walked through each
package with the maintenance crew doing the work. Quality control personnel were
l
present whenever required by the work order plans and quality control hold points were
properly verified and signed off.
i
!
l
The maintenance crews used self-verification checks in the cramped and sensitive work
j
environment. Workers also displayed good questioning attitudes during the course of the
i
work. Worker-identified discrepancies in work plans were called to the attention of
l
maintenance supervision and corrected appropriately.
i
i
                                  properly verified and signed off.
l
l
c.
Conclusions
1
l
The inspectors concluded that the control board wire separation work was performed in a
,
professional and thorough manner, All work observed was performed with the
appropriate work order plan present and being appropriately referenced.
j
!
!
l                                The maintenance crews used self-verification checks in the cramped and sensitive work
M1.2 Unit 1 Reactor Vessel Lower intemals Lift
j                                environment. Workers also displayed good questioning attitudes during the course of the
a.
i                                 work. Worker-identified discrepancies in work plans were called to the attention of
Inspection Scope (IP 62707)
l                                maintenance supervision and corrected appropriately.
The inspectors observed the planning and execution of the Unit i reactor vessel (RV)
i                                                                                                                              l
i
l                    c.          Conclusions                                                                                  1
lower intemals lift.
b.
Obser<ations and Findinas -
The inspectors attended a work preparation briefing on March 3,1998, which was held to
discuss the various aspects of the lower intamals lifting evolution. Work group
l
l
                                  The inspectors concluded that the control board wire separation work was performed in a      ,
responsibilities were identified and Routine Maintenance Procedure (RMP) 9053, "RV
                                  professional and thorough manner, All work observed was performed with the                  l
Intemals Removal and Installation," Revision 1, was reviewed. Health physics
                                  appropriate work order plan present and being appropriately referenced.                      j
,
!                  M1.2 Unit 1 Reactor Vessel Lower intemals Lift
considerations were discussed; however, radiation work permits had not been completed.
                      a.        Inspection Scope (IP 62707)
'
                                  The inspectors observed the planning and execution of the Unit i reactor vessel (RV)        i
The inspectors made the following observations regarding the briefing:
                                  lower intemals lift.
Contrary to Nuclear Procedure 1.2.6, " Infrequently Performed Tests and
                      b.        Obser<ations and Findinas -
.
                                  The inspectors attended a work preparation briefing on March 3,1998, which was held to
Evolutions," Revision 4, the work activity was not categorized as an infrequently
                                  discuss the various aspects of the lower intamals lifting evolution. Work group
performed test or evolution. This condition was subsequently corrected prior to
l                                responsibilities were identified and Routine Maintenance Procedure (RMP) 9053, "RV
the beginning of work.
                                  Intemals Removal and Installation," Revision 1, was reviewed. Health physics                 ,
Health physics information discussed was not complete nor fully evaluated prior
                                  considerations were discussed; however, radiation work permits had not been completed.       '
.
                                  The inspectors made the following observations regarding the briefing:
to the planning meeting. For example, the radiation work permits had not been
                                  .      Contrary to Nuclear Procedure 1.2.6, " Infrequently Performed Tests and
prepared.
                                          Evolutions," Revision 4, the work activity was not categorized as an infrequently
l
                                          performed test or evolution. This condition was subsequently corrected prior to
Overall, discussions at the briefing (held 24 hours before the initiation of work)
                                          the beginning of work.
.
                                  .      Health physics information discussed was not complete nor fully evaluated prior
indicated that many aspects of the job had not been thoroughly evaluated.
                                          to the planning meeting. For example, the radiation work permits had not been
The initial attempt to lift the lower intemals was performed under the direction of a
                                          prepared.
maintenance supervisor. A senior manager was present in the containment to provide
l                                 .      Overall, discussions at the briefing (held 24 hours before the initiation of work)
oversight. The inspectors observed that the maintenance crew attached the containment
                                          indicated that many aspects of the job had not been thoroughly evaluated.
10
                                  The initial attempt to lift the lower intemals was performed under the direction of a
                                  maintenance supervisor. A senior manager was present in the containment to provide
                                  oversight. The inspectors observed that the maintenance crew attached the containment
                                                                              10
t
t


    _-_ ______ - _ _       _ _ _ _ - _ _ _ _ - _ _ _ _ _ _ _ - - _ _ _ - _ _ _ - _ - _                       __-__
_-_ ______ - _ _
  .                 .
_ _ _ _ - _ _ _ _ - _ _ _ _ _ _ _ - - _ _ _ - _ _ _ - _ - _
                        '
_ _ - _ _
                      .
.
                          polar crane hook to the "intemals lift rig," a special lifting platform, without inserting a load
.
                          cell between the hook and lift rig, as required by Step 7.3.7.f. of the RMP. The purpose
'
                          of the load cell was to provide early indication of binding during crane load vertical
.
                          movement. The inspectors asked the maintenance supervisor why this step had not
polar crane hook to the "intemals lift rig," a special lifting platform, without inserting a load
                          been completed. The supervisor stated that the lift rig was to be moved to the other side
cell between the hook and lift rig, as required by Step 7.3.7.f. of the RMP. The purpose
                          of the containment and the load cell would then be installed. This action would have
of the load cell was to provide early indication of binding during crane load vertical
                          been acceptable, since the procedure specifically only prevented the lifting rig from being
movement. The inspectors asked the maintenance supervisor why this step had not
                          positioned above the reactor vessel without the installed load cell. However, the crew
been completed. The supervisor stated that the lift rig was to be moved to the other side
l                         proceeded with positioning the lift rig above the RV with the intent of lowering the lift rig
of the containment and the load cell would then be installed. This action would have
                          into place on the RV and then installing the load cell. Positioning the intemals lift rig
been acceptable, since the procedure specifically only prevented the lifting rig from being
                          above the reactor vessel without the load cell installed was a violation
positioned above the reactor vessel without the installed load cell. However, the crew
                          (VIO 50-266/98006-02(DRP)) of T/S 15.6.81 for failure to follow procedures. Prior to the
l
                          lift rig being lowered onto the RV, the senior manager in containment recognized that the
proceeded with positioning the lift rig above the RV with the intent of lowering the lift rig
                          procedural requirements were being violated and stopped work. The action was
into place on the RV and then installing the load cell. Positioning the intemals lift rig
                          documented on CR 98-0831. A temporary change was made to RMP 9053 to allow
above the reactor vessel without the load cell installed was a violation
                          installation of the load cell after the lift rig was landed on the RV While the procedure
(VIO 50-266/98006-02(DRP)) of T/S 15.6.81 for failure to follow procedures. Prior to the
                          change was being processed, involved maintenance personnel stated that the original
lift rig being lowered onto the RV, the senior manager in containment recognized that the
                          procedure had been ir;dequate. The inspectors concluded that the steps in the original
procedural requirements were being violated and stopped work. The action was
                          procedure could have been performed as written. Additionally, the inspectors noted that
documented on CR 98-0831. A temporary change was made to RMP 9053 to allow
                          maintenance staff had ample opportunity during the pre-job briefing to decide how to
installation of the load cell after the lift rig was landed on the RV While the procedure
change was being processed, involved maintenance personnel stated that the original
procedure had been ir;dequate. The inspectors concluded that the steps in the original
procedure could have been performed as written. Additionally, the inspectors noted that
maintenance staff had ample opportunity during the pre-job briefing to decide how to
perform the steps as written or to identify attemate ways to perform the lift, and make any
,
,
                          perform the steps as written or to identify attemate ways to perform the lift, and make any
necessary procedural changes.
                          necessary procedural changes.
The maintenance crew attempted to lower the lift rig onto the RV after the temporary
                        The maintenance crew attempted to lower the lift rig onto the RV after the temporary
change was processed for the RMP. The three guide bushings on the lift rig were not
                          change was processed for the RMP. The three guide bushings on the lift rig were not
proper 1y aligned with the three guide studs in the RV flange, and at least one bushing was
                          proper 1y aligned with the three guide studs in the RV flange, and at least one bushing was
observed to be resting on the corresponding guide tube. The full weight of the lift rig
                          observed to be resting on the corresponding guide tube. The full weight of the lift rig
appeared to be placed on the guide bushings which were resting on top of the guide
                          appeared to be placed on the guide bushings which were resting on top of the guide
studs. The crane operator could not quickly identify the misalignment because the load
                          studs. The crane operator could not quickly identify the misalignment because the load
cell was not present to indicate reduced weight on the crane as the crane hook was
                          cell was not present to indicate reduced weight on the crane as the crane hook was
lowered. The lift rig was raised off the guide studs and rotated into proper alignment. On
                          lowered. The lift rig was raised off the guide studs and rotated into proper alignment. On
the second attempt at lowering the !ift rig, the mounting plates for two of the guide
                        the second attempt at lowering the !ift rig, the mounting plates for two of the guide
bushings were found to have been knocked out of alignment to the extent that the guide
                          bushings were found to have been knocked out of alignment to the extent that the guide
bushings would no longer slide down the guide studs. The lift rig was transferred back to
                          bushings would no longer slide down the guide studs. The lift rig was transferred back to
a laydown area, and the guide bushing mounting plates were realigned. Lifting
                          a laydown area, and the guide bushing mounting plates were realigned. Lifting
operations were suspended to allow for a shift change of personnel.
                          operations were suspended to allow for a shift change of personnel.
A pre-job briefing was conducted for the on-coming shift personnel. Overall, the briefing
                        A pre-job briefing was conducted for the on-coming shift personnel. Overall, the briefing
was conducted well. The maintenance supervisor in charge of the evolution displayed a
                        was conducted well. The maintenance supervisor in charge of the evolution displayed a
clear understanding of the task and clearly outlined roles and responsibilities of the work
                          clear understanding of the task and clearly outlined roles and responsibilities of the work       ,
,
                                                                                                                            '
'
                          crew members. During the conduct of the intemals lift, the maintenance supervisor
crew members. During the conduct of the intemals lift, the maintenance supervisor
                          maintained a " big picture" oversight of the activity. Having noted the procedural
maintained a " big picture" oversight of the activity. Having noted the procedural
                          compliance problems during the previous shift, the work crew leader was deliberate in
compliance problems during the previous shift, the work crew leader was deliberate in
                        taking actions and frequently referenced the RMP to ensure steps were appropriately
taking actions and frequently referenced the RMP to ensure steps were appropriately
                          completed. The lift was conducted very methodically and was controlled well. The lower
completed. The lift was conducted very methodically and was controlled well. The lower
                          intemals were placed in the storage area of the Unit 1 cavity area without incident.
intemals were placed in the storage area of the Unit 1 cavity area without incident.
                                                                                        11
11


                                  _ _ - _ _     _ -___-_ _ _ _ _ ______ _ _ - - __ _                                 --
_ _ - _ _
  . .
_ -___-_ _ _ _ _ ______ _ _ - - __ _
              -
--
      .
.
        c.     Conclusions
.
                The inspectors concluded that the maintenance and health physics organizations were
-
                not adequately prepared to perform the lower intemals lift based on planning meetings
.
                conducted 24 hours prior to the initiation of work. In addition, early in the evolution, the
c.
                inspectors identified a failure of maintenance workers to follow procedures as required by
Conclusions
                T/S. This was considered a violation. Later in the evolution, the maintenance
The inspectors concluded that the maintenance and health physics organizations were
                organization displayed better control of the activity and the lower internals were moved
not adequately prepared to perform the lower intemals lift based on planning meetings
                without incident.
conducted 24 hours prior to the initiation of work. In addition, early in the evolution, the
        M1.3 Inconsistent Application of Administrative Controls in Maintenance
inspectors identified a failure of maintenance workers to follow procedures as required by
        a.     Inspection Scope (IPs 62707 and 40500)
T/S. This was considered a violation. Later in the evolution, the maintenance
                The inspectors assessed the maintenance department's implementation of administrative
organization displayed better control of the activity and the lower internals were moved
                controls, including procedure adherence.
without incident.
        b.     Observations and Findinas
M1.3 Inconsistent Application of Administrative Controls in Maintenance
                Maintenance personnel were observed to be performing many maintenance activities in
a.
                full compliance with procedural and other administrative controls. However, the failure to
Inspection Scope (IPs 62707 and 40500)
                utilize the procedural controls in place during the lower intemals lift, and the failure to
The inspectors assessed the maintenance department's implementation of administrative
                effectively utilize the pre-job brief to ensure the appropriateness of the planned method of               )
controls, including procedure adherence.
                performing work during the lower intemals lift, described in Section M1.2 above, were
b.
                indicative of inconsistencies in the maintenance department's application of standard
Observations and Findinas
                administrative controls. The inspectors identified two other minor discrepancies in the
Maintenance personnel were observed to be performing many maintenance activities in
                application of administrative controls by the maintenance department during this period.
full compliance with procedural and other administrative controls. However, the failure to
                These conditions were discussed with licensee staff and were corrected under
utilize the procedural controls in place during the lower intemals lift, and the failure to
                CR 98-0917 and CR 98-1168. Additional,' unrelated examples of inconsistent application
effectively utilize the pre-job brief to ensure the appropriateness of the planned method of
                of administrative controls were identified by the licensee, and were documented in
)
                CR 98-1369 ar~i CR 98-1463. Similar issues were discussed in Section M2.2 of
performing work during the lower intemals lift, described in Section M1.2 above, were
                IR No. 50-266i98003(DRP); 50-301/98003(DRP).
indicative of inconsistencies in the maintenance department's application of standard
                                                                                                                          l
administrative controls. The inspectors identified two other minor discrepancies in the
                Specific corrective actions were taken for each identified discrepancy, but the inspectors
application of administrative controls by the maintenance department during this period.
                noted that there was no broad-based initiative to address the observed discrepancies.                     j
These conditions were discussed with licensee staff and were corrected under
                Additionally, some of the corrective actions were narrowly focused. For instance, the only
CR 98-0917 and CR 98-1168. Additional,' unrelated examples of inconsistent application
                corrective action documented for the RV lower intemals lift procedure violation
of administrative controls were identified by the licensee, and were documented in
                (CR 98-0831) was a permanent change to the procedure to add greater flexibility in the
CR 98-1369 ar~i CR 98-1463. Similar issues were discussed in Section M2.2 of
                performance of work steps. This did not appear to address all of the performance issues
IR No. 50-266i98003(DRP); 50-301/98003(DRP).
                discussed in Section M1.2 above. This concem was discussed with the maintenance
l
;.              manager, who indicated that the performance discrepancies were not pervasive, and that
Specific corrective actions were taken for each identified discrepancy, but the inspectors
i              various initiatives were in place to improve the performance of maintenance activities.
noted that there was no broad-based initiative to address the observed discrepancies.
                The maintenance manager further stated that a coordinated effort to address both long-
j
!.             term corrective actions and interim actions within the department was worth
Additionally, some of the corrective actions were narrowly focused. For instance, the only
corrective action documented for the RV lower intemals lift procedure violation
(CR 98-0831) was a permanent change to the procedure to add greater flexibility in the
performance of work steps. This did not appear to address all of the performance issues
discussed in Section M1.2 above. This concem was discussed with the maintenance
manager, who indicated that the performance discrepancies were not pervasive, and that
;.
various initiatives were in place to improve the performance of maintenance activities.
i
The maintenance manager further stated that a coordinated effort to address both long-
!.
term corrective actions and interim actions within the department was worth
consideration.
'
'
                consideration.
c.
        c.    Conclusions
Conclusions
                Many of the maintenance activities observed were completed in accordance with
Many of the maintenance activities observed were completed in accordance with
                requirements specified in administrative and work control procedures. However, the
requirements specified in administrative and work control procedures. However, the
                                                                                    12
12
                                                                                        _ _ _ _ _ _ _ _ _ _ - _ - _ _   -
_ _ _ _ _ _ _ _ _ _ - _ - _ _
-


      -_-   _     -     - _ _ _ - _ _ _ _ _ _ _ _ - - _ _ _ - _ _ _ _ _ - _ _ _ _ - _ _ _ - _ _ - _ - _ _ _ _ _ _ _ - _ _ - _ _ _
-_-
  . .
_
                  .
-
                  inspectors noted cases where administrative requirements were not being implemented.
- _ _ _ - _ _ _ _ _ _ _ _ - - _ _ _ - _ _ _ _ _ - _ _ _ _ - _ _ _ - _ _ - _ - _ _ _ _ _ _ _ - _ _ - _ _ _
l                 The licensee's corrective action program also identified similar examples of this problem.
.
                  Some of the corrective actions for these issues were narrowly focused and lacked an
.
                  integrated effort to address the inconsistencies in application of administrative controls                           i
.
                  within the maintenance department.
inspectors noted cases where administrative requirements were not being implemented.
          M1.4 Troubleshooting a Breaker Indication Failure
l
The licensee's corrective action program also identified similar examples of this problem.
Some of the corrective actions for these issues were narrowly focused and lacked an
integrated effort to address the inconsistencies in application of administrative controls
i
within the maintenance department.
M1.4 Troubleshooting a Breaker Indication Failure
l
The inspectors reviewed the licensee's troubleshooting and corrective actions for a failure
of the control room indication for motor-driven auxiliary feedwater pump P-38A. The
associated work order Packages 9708867 and 9804735 were complete and thorough.
No administrative or technical concems were identified.
M1.5 Freeze Seal for Repair of Component Coolina Water Check Valve. 2CC-745 (IP 61707)
The licensee used a freeze seal to assist in the performance of a visual inspection and
repair of 2CC-745. The inspectors verified that the licensee had taken appropriate
measures to address industry-related problems with freeze seals. Maintenance
Procedure RMP 9327, "CC-745 Swing Check Vane Inspection," Revision 0, and
10 CFR 50.59 safety evaluation (SE) 98-037 contained requirements that reflected these
l
l
                  The inspectors reviewed the licensee's troubleshooting and corrective actions for a failure
measures and were determined to be adequate by the inspectors.
                  of the control room indication for motor-driven auxiliary feedwater pump P-38A. The
'
                  associated work order Packages 9708867 and 9804735 were complete and thorough.
                  No administrative or technical concems were identified.
                                                                                                                                      I
          M1.5 Freeze Seal for Repair of Component Coolina Water Check Valve. 2CC-745 (IP 61707)
                  The licensee used a freeze seal to assist in the performance of a visual inspection and
                  repair of 2CC-745. The inspectors verified that the licensee had taken appropriate
                  measures to address industry-related problems with freeze seals. Maintenance
                  Procedure RMP 9327, "CC-745 Swing Check Vane Inspection," Revision 0, and
                  10 CFR 50.59 safety evaluation (SE) 98-037 contained requirements that reflected these                              l
l                measures and were determined to be adequate by the inspectors.                                                       '
l
l
                  The inspectors attended the maintenance and operations department freeze seal pre-
l~
l~                evolution briefings held on March 17,1998. The briefings were thorough and covered
The inspectors attended the maintenance and operations department freeze seal pre-
                  command and control responsibilities, expected communication standards, and                                         i
evolution briefings held on March 17,1998. The briefings were thorough and covered
                                                                                                                                        '
command and control responsibilities, expected communication standards, and
i                 contingencies. Teamwork between the different disciplines was evident and participants
i
i                 displayed a good questioning attitude. The licensee completed inspection and repair of                               l
'
i
contingencies. Teamwork between the different disciplines was evident and participants
i
displayed a good questioning attitude. The licensee completed inspection and repair of
!
!
                  2CC-745 as planned.
2CC-745 as planned.
l
l
!
!
          M8     Miscellaneous Maintenance issues
M8
          M8.1 (Closed) LER 50-301/95006: PORV (Power-Operated Relief Valve) Post-Maintenance
Miscellaneous Maintenance issues
l                 Testing Not Performed Prior to Establishing LTOP (Low Temperature Over-Pressure
M8.1 (Closed) LER 50-301/95006: PORV (Power-Operated Relief Valve) Post-Maintenance
l                 Protection). The licensee identified that LTOP was not properly established after the
l
i                 reactor vessel head was reinstalled because one of two PORVs required for LTOP was
Testing Not Performed Prior to Establishing LTOP (Low Temperature Over-Pressure
                  inoperable. The valve was considered inoperable because post-maintenance testing had
l
                  not been completed. A root cause evaluation by the licensee identified that a
Protection). The licensee identified that LTOP was not properly established after the
i
reactor vessel head was reinstalled because one of two PORVs required for LTOP was
inoperable. The valve was considered inoperable because post-maintenance testing had
not been completed. A root cause evaluation by the licensee identified that a
l
misunderstanding in the work control center resulted in the post-maintenance test for the
l
l
                  misunderstanding in the work control center resulted in the post-maintenance test for the
valve not being performed before the reactor head was reinstalled. With the reactor head
l                valve not being performed before the reactor head was reinstalled. With the reactor head
installed, LTOP was required. In addition, control room operators were unaware that the
                  installed, LTOP was required. In addition, control room operators were unaware that the
l
l
                  post-maintenance test had not been completed.
post-maintenance test had not been completed.
                  Two operable PORVs were required for LTOP, but the T/S allowed one valve to be
Two operable PORVs were required for LTOP, but the T/S allowed one valve to be
!                 inoperable for a limited time period. The licensee was allowed 24 hours to restore the
!
inoperable for a limited time period. The licensee was allowed 24 hours to restore the
!
!
                  inoperable PORV and an additional 8 hours to depressurize and vent the reactor coolant
inoperable PORV and an additional 8 hours to depressurize and vent the reactor coolant
                  system if the PORV could not be made operable. However, the valve was inoperable for
system if the PORV could not be made operable. However, the valve was inoperable for
                  about 34 hours and the reactor coolant system had not been depressurized or vented.
about 34 hours and the reactor coolant system had not been depressurized or vented.
                  Licensee management counseled operators and work control center staff on the
Licensee management counseled operators and work control center staff on the
                  inappropriate delay in completing the post-maintenance test and revised several
inappropriate delay in completing the post-maintenance test and revised several
                                                                                                                                    13
13


  _   ._ . _ _ _ _ _ _ _ .             _
_
                                            _ _ _ _ _ _ _ _ - - _ _ _ _ _ _ _ - _ _ _ _ _ _ _ _ _ _ _ - - _ _ _ - _ _ _ -
._ . _ _ _ _ _ _ _ .
    .                 .
_
                                -
_ _ _ _ _ _ _ _ - - _ _ _ _ _ _ _ - _ _ _ _ _ _ _ _ _ _ _ - - _ _ _ - _ _ _ -
                          .
.
                                  procedures to highlight the need for PORV operability (and establishing LTOP) prior to
.
                                  reactor head installation. The problem has not reoccurred and an extensive review of the
-
                                  post-maintenance testing process by the licensee in the past year, with concurrent NRC
.
                                  monitoring of that review (see, for example, Sections M1.1 and M3.1 of
procedures to highlight the need for PORV operability (and establishing LTOP) prior to
                                  IR No. 50-266/97010(DRS); 50-301/97010(DRS), has given further assurance that this
reactor head installation. The problem has not reoccurred and an extensive review of the
                                  will remain an isolated event. This licensee-identified and corrected violation is being
post-maintenance testing process by the licensee in the past year, with concurrent NRC
                                  treated as a non-cited violation (NCV 50-301/98006-03(DRP)), consistent with
monitoring of that review (see, for example, Sections M1.1 and M3.1 of
                                  Section Vll.B.1 of the NRC Enforcement Policy.
IR No. 50-266/97010(DRS); 50-301/97010(DRS), has given further assurance that this
                          M8.2 (Closed) IFl 50-266/%002-01(DRP): 50-301/96002-01(DRP): This IFl comprised several
will remain an isolated event. This licensee-identified and corrected violation is being
                                  inspector concems generally related to work planning and scheduling. One of those
treated as a non-cited violation (NCV 50-301/98006-03(DRP)), consistent with
                                  concems was that an SE which addressed equipment operability could be prepared and
Section Vll.B.1 of the NRC Enforcement Policy.
                                  approved without control room personnel being made aware of possible changes to the
M8.2 (Closed) IFl 50-266/%002-01(DRP): 50-301/96002-01(DRP): This IFl comprised several
                                  operability status of plant equipment specified in the SE. Because of this and other
inspector concems generally related to work planning and scheduling. One of those
                                  problems with the SE process, the licensee reviewed numerous existing SEs, extensively
concems was that an SE which addressed equipment operability could be prepared and
l                                 restructured the goveming procedure for conducting an SE, trained plant staff on the
approved without control room personnel being made aware of possible changes to the
                                  revised procedure, and established a multi-disciplinary team of which a member would
operability status of plant equipment specified in the SE. Because of this and other
                                  review all SE screenings. Recent NRC inspections (irs No. 50-266/97010(DRS);
problems with the SE process, the licensee reviewed numerous existing SEs, extensively
                                  50-301/97010(DRS) and No. 50-266/97023(DRS); 50-301/97023(DRS)) have identified
l
                                  that the SE process has improved. The original concem of this IFl has been adequately
restructured the goveming procedure for conducting an SE, trained plant staff on the
                                  addressed.
revised procedure, and established a multi-disciplinary team of which a member would
                                  A second concem pertained to the concurrent use of a CCW pump as the redundam
review all SE screenings. Recent NRC inspections (irs No. 50-266/97010(DRS);
                                  pump for two other CCW pumps. This concem was adequately addressed with the
50-301/97010(DRS) and No. 50-266/97023(DRS); 50-301/97023(DRS)) have identified
                                  revision (in June 1997) of T/S 15.3.3.C. for the CCW pumps. This revision removed the
that the SE process has improved. The original concem of this IFl has been adequately
                                  previous ambiguity on redundant pumps and does not allow the use of a CCW pump
addressed.
                                  assigned to one Unit as a redundant pump for the other Unit.                               ,
A second concem pertained to the concurrent use of a CCW pump as the redundam
pump for two other CCW pumps. This concem was adequately addressed with the
revision (in June 1997) of T/S 15.3.3.C. for the CCW pumps. This revision removed the
previous ambiguity on redundant pumps and does not allow the use of a CCW pump
assigned to one Unit as a redundant pump for the other Unit.
,
The remaining two items pertained specifically to poor planning and scheduling of work
'
'
                                  The remaining two items pertained specifically to poor planning and scheduling of work
on an emergency diesel generator (EDG) and a CCW pump. Recent inspection reports
                                  on an emergency diesel generator (EDG) and a CCW pump. Recent inspection reports
(irs No. 50-266/97003(DRP); 50-301/97003(DRP), No. 50-266/97006(DRP);
                                  (irs No. 50-266/97003(DRP); 50-301/97003(DRP), No. 50-266/97006(DRP);
50-301/97006(DRP), No. 50-266/97013(DRP); 50-301/97013(DRP), and
                                  50-301/97006(DRP), No. 50-266/97013(DRP); 50-301/97013(DRP), and
No. 50-266/97021(DRP); 50-301/97021(DRP)) document additionalinstances of poor
                                  No. 50-266/97021(DRP); 50-301/97021(DRP)) document additionalinstances of poor
work planning and scheduling. Although none of these items involved violations of NRC
                                  work planning and scheduling. Although none of these items involved violations of NRC
requirements, they indicated that the work planning and scheduling process was weak
                                  requirements, they indicated that the work planning and scheduling process was weak
As discussed in IR No. 50-266/97006(DRP); 50-301/97006(DRP), the licensee has
                                  As discussed in IR No. 50-266/97006(DRP); 50-301/97006(DRP), the licensee has
recently undertaken several initiatives following an extensive maintenance program
                                  recently undertaken several initiatives following an extensive maintenance program
improvement review. Because the implementation of these programmatic initiatives is
                                  improvement review. Because the implementation of these programmatic initiatives is
being tracked as an IFl (50-266/97006-02(DRP); 50-301/97006-02(DRP)) and the original
                                  being tracked as an IFl (50-266/97006-02(DRP); 50-301/97006-02(DRP)) and the original
SE and CCW concems discussed above have been adequately addressed, the two
                                  SE and CCW concems discussed above have been adequately addressed, the two
concerns about specific work planning and scheduling problems are considered closed.
                                  concerns about specific work planning and scheduling problems are considered closed.
M8.3 (Closed) LER 50-266/97042: Failure to perform containment personnel air lock
                          M8.3 (Closed) LER 50-266/97042: Failure to perform containment personnel air lock
surveillance while door interlock is inoperable. The events and circumstances of this LER
                                  surveillance while door interlock is inoperable. The events and circumstances of this LER
were discussed in IR No. 50-266/97021(DRP); 50-301/97021(DRP), Section M2.1. A
                                  were discussed in IR No. 50-266/97021(DRP); 50-301/97021(DRP), Section M2.1. A
Notice of Violation was issued regarding this matter. Therefore, this LFR is considered
                                  Notice of Violation was issued regarding this matter. Therefore, this LFR is considered
l
l                                 closed with the existing open violation (VIO 50-266/97021-02(DRP);
closed with the existing open violation (VIO 50-266/97021-02(DRP);
i                                 50-301/97021-02(DRP)) serving as the inspection tracking mechanism for completion of
i
                                  the corrective actions.                                                                     .
50-301/97021-02(DRP)) serving as the inspection tracking mechanism for completion of
                                                                                                                              I
the corrective actions.
                                                                                                                                i
.
                                                                                                                          14
I
                                                                                                                                i
i
14
i


- - - _ - _ _ - _ - _ - - - - _ _ - - - _ _                                                                                                               -- -       _-               -         _
- - - _ - _ _ - _ - _ - - - - _ _ - - - _ _
                  .                       .                                                                                                                                                     ;
-- -
                                                                                                      -
_-
                                                    .
-
                                                                                                                                          lil. Enaineerina
_
                                                E1                                                   Conduct of Engineering                                                                       l
;
                                                                                                                                                                                                  l
.
                                                E1.1                                                 EDG Room Ventilation System Safety Classification
.
                                                          a.                                         Inspection Scope UP 37551)
-
                                                                                                      The inspectors reviewed aspects of the safety classification of the EDG room ventilation
.
                                                                                                      systems.
lil. Enaineerina
                                                          b.                                         Observations and Findinas
E1
                                                                                                      The inspectors reviewed the safety classification of the G-01 and G-02 EDG room
Conduct of Engineering
                                                                                                      ventilation system components. This review was performed while independently
E1.1
                                                                                                      assessing the technical merits of an OD associated with EDG output ratings at elevated
EDG Room Ventilation System Safety Classification
                                                                                                      room temperatures. The inspectors noted that the G-01 exhaust fan control panel
a.
                                                                                                      (C-032) was classified as safety-related; however, the G-02 exhaust fan control panel
Inspection Scope UP 37551)
                                                                                                      (C-036) was classified as nonsafety-related. The inspectors questioned the system
The inspectors reviewed aspects of the safety classification of the EDG room ventilation
                                                                                                      engineer about this difference. After reviewing the component history, the system
systems.
                                                                                                      engineer determined that the list of safety-related components had not been appropriately
b.
                                                                                                      updated to add C-036 as committed to in LER 50-301/91001-01. This problem was
Observations and Findinas
                                                                                                      documented in CR 98-1084.
The inspectors reviewed the safety classification of the G-01 and G-02 EDG room
                                                                                                      The inspectors reviewcd the corrective actions for CR 98-1084 to ensure that the issue
ventilation system components. This review was performed while independently
                                                                                                      had been adequately addressed. The corrective actions consisted of a broad review of
assessing the technical merits of an OD associated with EDG output ratings at elevated
                                                                                                      the EDG room ventilation system to determine whether any other discrepancies existed,
room temperatures. The inspectors noted that the G-01 exhaust fan control panel
                                                                                                      and a review to determine whether the condition was reportable. While these two
(C-032) was classified as safety-related; however, the G-02 exhaust fan control panel
                                                                                                      corrective actions were appropriate, both the CR and the corrective action documents
(C-036) was classified as nonsafety-related. The inspectors questioned the system
                                                                                                      specified that the as-found condition was administrative in nature. The problem could
engineer about this difference. After reviewing the component history, the system
                                                                                                      have been more substantial had the appropriate configuration and material controls not
engineer determined that the list of safety-related components had not been appropriately
                                                                                                      been maintained between the time C-036 was dedicated as being safety-related and the
updated to add C-036 as committed to in LER 50-301/91001-01. This problem was
                                                                                                      identification of the error. The inspectors communicated this concem to the appropriate
documented in CR 98-1084.
                                                                                                      system engineering supervisor, who initiated an additional corrective action to review the
The inspectors reviewcd the corrective actions for CR 98-1084 to ensure that the issue
                                                                                                      maintenance and modification history of C-036 to ensure that its configuration and
had been adequately addressed. The corrective actions consisted of a broad review of
                                                                                                      material status had not been compromised. No problems were identified during this
the EDG room ventilation system to determine whether any other discrepancies existed,
                                                                                                      review.
and a review to determine whether the condition was reportable. While these two
                                                                                                                                                                                                  1
corrective actions were appropriate, both the CR and the corrective action documents
                                                                                                      The inspectors considered the safety significance of this specific issue to be minor;
specified that the as-found condition was administrative in nature. The problem could
                                                                                                      therefore, the failure to implement effective corrective actions regarding the safety
have been more substantial had the appropriate configuration and material controls not
                                                                                                      classification of C-036 (with respect to LER 50-301/91001-01 and CR 98-1084) was a
been maintained between the time C-036 was dedicated as being safety-related and the
                                                                                                    . non-cited violation (NCV 50-301/98006-04) of 10 CFR Part 50, Appendix B, Criterion XVI,
identification of the error. The inspectors communicated this concem to the appropriate
                                                                                                      " Corrective Action," consistent with Section IV of the NRC Enforcement Policy.
system engineering supervisor, who initiated an additional corrective action to review the
                                                          c.                                         Conclusions
maintenance and modification history of C-036 to ensure that its configuration and
                                                                                                      The inspectors identified a minor discrepancy in the licensee's list of safety-related
material status had not been compromised. No problems were identified during this
                                                                                                      components. Specifically, a ventilation control panel in an EDG room was misclassified.
review.
                                                                                                      The licensee's initial corrective actions did not include determining if the ventilation
1
                                                                                                      system operability had been challenged while the component was incorrectly classified as
The inspectors considered the safety significance of this specific issue to be minor;
                                                                                                                                                  15
therefore, the failure to implement effective corrective actions regarding the safety
        -_                                   _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ - _ _ _ _ _ _ _ __-__
classification of C-036 (with respect to LER 50-301/91001-01 and CR 98-1084) was a
. non-cited violation (NCV 50-301/98006-04) of 10 CFR Part 50, Appendix B, Criterion XVI,
" Corrective Action," consistent with Section IV of the NRC Enforcement Policy.
c.
Conclusions
The inspectors identified a minor discrepancy in the licensee's list of safety-related
components. Specifically, a ventilation control panel in an EDG room was misclassified.
The licensee's initial corrective actions did not include determining if the ventilation
system operability had been challenged while the component was incorrectly classified as
15
- _
_ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ - _ _ _ _ _ _ _ __-__


                                                                                                                          J
J
  .                     .
.
                                .
.
                                being nonsafety-related. Subsequent review indicated no problems in this area and the
.
                                discrepancy was corrected.
being nonsafety-related. Subsequent review indicated no problems in this area and the
                          E1.2 Seismic Isolation in Pipina Systems
discrepancy was corrected.
                            a. Inspection Scope (IP 92700)
E1.2
                                The inspectors reviewed two LERs that dealt with discrepancies conceming the
Seismic Isolation in Pipina Systems
                                conformance of plant piping systems to Final Safety Analysis Report (FSAR)
a.
                                commitments.
Inspection Scope (IP 92700)
                            b. Observations and Findinas
The inspectors reviewed two LERs that dealt with discrepancies conceming the
                                Licensee Event Report 50-266/97021 documented the failure to maintain two valves in
conformance of plant piping systems to Final Safety Analysis Report (FSAR)
                                the spent fuel pool (SFP) cooling system in a normally closed position. These two valves
commitments.
                                separated seismically qualified portions of the SFP cooling system from non-seismically
b.
                                qualified portions of the system. Licensee Event Report 50-266/97028 documented that
Observations and Findinas
                                piping which was not seismically qualified was connected to the seismically qualified
Licensee Event Report 50-266/97021 documented the failure to maintain two valves in
                                refueling water storage tank (RWST) by way of normally open valves. The FSAR requires
the spent fuel pool (SFP) cooling system in a normally closed position. These two valves
                                that valves which separate seismically qualified from non-seismically qualified systems be
separated seismically qualified portions of the SFP cooling system from non-seismically
                                normally closed.                                                                           i
qualified portions of the system. Licensee Event Report 50-266/97028 documented that
                                The licensee initiated a broad assessment of a!I systems which contained a seismically
piping which was not seismically qualified was connected to the seismically qualified
                                qualified to non-qualified interface. Corrective actions were planned for all pipe systems
refueling water storage tank (RWST) by way of normally open valves. The FSAR requires
                                where adequate system separation did not exist. These actions were discussed with the       j
that valves which separate seismically qualified from non-seismically qualified systems be
                                NRC during public meetings and were documented in docketed letters to the NRC dated
normally closed.
                                July 25,1997 (NPL 97-0432), and December 19,1997 (NPL 97-0803). The inspectors             l
The licensee initiated a broad assessment of a!I systems which contained a seismically
                                reviewed the documentation associated with this issue and considered the docketed
qualified to non-qualified interface. Corrective actions were planned for all pipe systems
                                information to be accurate and comprehensive. The corrective actions were considered
where adequate system separation did not exist. These actions were discussed with the
                                to be appropriate. This licensee-identified and corrected, non-repetitive failure to
j
                                maintain the SFP cooling system and RWST recirculation pipe isolation valves in the
NRC during public meetings and were documented in docketed letters to the NRC dated
                                design position (normally closed), was a non-cited violation (NCV 50-266/98006-05(DRP);
July 25,1997 (NPL 97-0432), and December 19,1997 (NPL 97-0803). The inspectors
                                50-301/98006-05(DRP)) of 10 CFR Part 50, Appendix B, Criterion lil, " Design Control,"
reviewed the documentation associated with this issue and considered the docketed
                                cor.sistent with Section Vll.B.1 of the NRC Enforcement Policy,
information to be accurate and comprehensive. The corrective actions were considered
                            c. C_o nclusions
to be appropriate. This licensee-identified and corrected, non-repetitive failure to
                                The licensee identified and implemented effective corrective actions for two cases where
maintain the SFP cooling system and RWST recirculation pipe isolation valves in the
                                valves between seismically qualified piping systems and non-qualified piping systems
design position (normally closed), was a non-cited violation (NCV 50-266/98006-05(DRP);
                                were not maintained in a closed position as required by the FSAR.
50-301/98006-05(DRP)) of 10 CFR Part 50, Appendix B, Criterion lil, " Design Control,"
                          E1.3 Maintaining Desian Basis Inteority                                                         l
cor.sistent with Section Vll.B.1 of the NRC Enforcement Policy,
C_ nclusions
o
c.
The licensee identified and implemented effective corrective actions for two cases where
valves between seismically qualified piping systems and non-qualified piping systems
were not maintained in a closed position as required by the FSAR.
E1.3
Maintaining Desian Basis Inteority
l
a.
Inspection Scope (IP 37551)
l
l
                            a.  Inspection Scope (IP 37551)
l
l
l                              The inspectors reviewed the current status of licensee actions to ensure conformance of
The inspectors reviewed the current status of licensee actions to ensure conformance of
                                plant piping systems to FSAR commitments.
plant piping systems to FSAR commitments.
                                                                          16
16
[-   _ _ _ _ _ _ _ _ - -
[-
_ _ _ _ _ _ _ _ - -


  ,   ,
,
          a
,
                                                                                                                j
a
            b.   Observations and Findinas                                                                     )
j
                  The inspectors discussed the status of the licensee's ongoing assessments of the
b.
                  adequacy of the separation of seismically qualified and non-qualified piping systems with
Observations and Findinas
                  the cognizant design engineering personnel. The engineers described the screening
)
                  process being used to determine whether various systems were in conformance with the
The inspectors discussed the status of the licensee's ongoing assessments of the
                  FSAR commitments, and whether modifications would be required for systems and
adequacy of the separation of seismically qualified and non-qualified piping systems with
                  components which were operable, but not in compliance with the existing FSAR. The
the cognizant design engineering personnel. The engineers described the screening
                  screening criteria included the identification of motor-operated valves and check valves
process being used to determine whether various systems were in conformance with the
                  which could serve the function of a normally closed valva. When such motor-operated
FSAR commitments, and whether modifications would be required for systems and
                  valves or check valves existed, additional corrective actions for those systems were not
components which were operable, but not in compliance with the existing FSAR. The
                  considered necessary to address the seismically qualified to non-qualified separation
screening criteria included the identification of motor-operated valves and check valves
                  concem. However, the criteria did not require the evaluation of whether such motor-
which could serve the function of a normally closed valva. When such motor-operated
                  operated valves or check valves were considered seismic-class boundsry valves in the
valves or check valves existed, additional corrective actions for those systems were not
                  system design and licensing bases.
considered necessary to address the seismically qualified to non-qualified separation
                  The inspectors asked whether the screening criteria had been discussed with the onsite
concem. However, the criteria did not require the evaluation of whether such motor-
                  licensee staff performing rebaselining reviews of the inservice testing (IST) program and
operated valves or check valves were considered seismic-class boundsry valves in the
                  the FSAR. The engineers inrifcated that such discussions had not taken place. The
system design and licensing bases.
I                 inspectors subsequently determined that the IST and inservice inspection programs could
The inspectors asked whether the screening criteria had been discussed with the onsite
                  have been affected by the seismic review program screening criteria, and that the IST         ;
licensee staff performing rebaselining reviews of the inservice testing (IST) program and
                                                                                                                '
the FSAR. The engineers inrifcated that such discussions had not taken place. The
                  system engineer had not been aware of the seismic review until after the inspectors
I
                  questioned the design engineering personnel. While this issue may have eventually been       i
inspectors subsequently determined that the IST and inservice inspection programs could
                  identified by the licensee through supervisory reviews of the results of this seismic review
have been affected by the seismic review program screening criteria, and that the IST
                                                                                                                '
;
l                program, the inspectors considered the failure to integrate the seismic review program
system engineer had not been aware of the seismic review until after the inspectors
'
questioned the design engineering personnel. While this issue may have eventually been
i
identified by the licensee through supervisory reviews of the results of this seismic review
l
program, the inspectors considered the failure to integrate the seismic review program
'
'
                  with the IST testing program review a weakness.
'
                  The licensee had several ongoing, parallel improvement initiatives which were in             l
with the IST testing program review a weakness.
                                                                                                                '
The licensee had several ongoing, parallel improvement initiatives which were in
                  response to previous NRC enforcement actions. These included development of design
response to previous NRC enforcement actions. These included development of design
                  basis documents, a verification and update of the FSAR, rebaselining the IST program,
'
                  reviewing the inservice inspection program, rewriting system operating procedures, and
basis documents, a verification and update of the FSAR, rebaselining the IST program,
                  updating the IST procedures. Changes in system design basis, such as the addition of a
reviewing the inservice inspection program, rewriting system operating procedures, and
                  safety-related function to an existing valve, brought about by licensee staff working on
updating the IST procedures. Changes in system design basis, such as the addition of a
                  one of these efforts, could negatively affect the other improvement initiatives if not
safety-related function to an existing valve, brought about by licensee staff working on
                  properly documented and coordinated. The inspectors reviewed the licensee's response
one of these efforts, could negatively affect the other improvement initiatives if not
                  to the latest Systematic Assessment of Licensee Performance, report
properly documented and coordinated. The inspectors reviewed the licensee's response
                  No. 50-266/97001; 50-301/97001, and found that the licensee acknowledged the need to
to the latest Systematic Assessment of Licensee Performance, report
;.               control design basis changes when making plant hardware changes, but that there was
No. 50-266/97001; 50-301/97001, and found that the licensee acknowledged the need to
l                 no specified initiative to control the effects of design basis changes that might occur as
;.
j                 the result of analysis or software changes.
control design basis changes when making plant hardware changes, but that there was
                  The inspectors met with senior licensee management to express the concem that design
l
                  engineering staff had been working on a committed corrective action for eleven months
no specified initiative to control the effects of design basis changes that might occur as
                  without coordinating their efforts with other interrelated corrective action initiatives. The
j
                  inspectors asked whether this was indicative of a broad problem in design engineering, or
the result of analysis or software changes.
                  was an isolated incident. The licensee managers acknowledged the inspectors' concem,
The inspectors met with senior licensee management to express the concem that design
                  and were reviewing the issue at the end of the inspection period. The inspectors will
engineering staff had been working on a committed corrective action for eleven months
                  track the licensee's actions to ensure that design basis changes, including those brought
without coordinating their efforts with other interrelated corrective action initiatives. The
                                                              17
inspectors asked whether this was indicative of a broad problem in design engineering, or
L_ _ _ _ _ _ - - __
was an isolated incident. The licensee managers acknowledged the inspectors' concem,
and were reviewing the issue at the end of the inspection period. The inspectors will
track the licensee's actions to ensure that design basis changes, including those brought
17
L      - -  


  __
__
    _ - _ _ _                 .__         _ _ _ _ _ -     _.
_ - _ _ _
                                                                  -___-____                          ___
.__
  .         .
_ _ _ _ _ -
                    -
_.
              .
- _ _ _ - _ _ _ _
                    about by analysis, are property documented and communicated as an inspection follow-
___
                    up item (IFl 50 266/98006-06(DRP); 50-301/98006-06(DRP)).
.
              c.   Conclusions
.
                    Offsite, corporate office-based engineering personnel working on a corrective action
-
!                   commitment initiative to assess the adequacy of a separation of seismically qualified and
.
                    non-qualified piping systems were performing analyses and taking credit for components
about by analysis, are property documented and communicated as an inspection follow-
up item (IFl 50 266/98006-06(DRP); 50-301/98006-06(DRP)).
c.
Conclusions
Offsite, corporate office-based engineering personnel working on a corrective action
!
commitment initiative to assess the adequacy of a separation of seismically qualified and
l
non-qualified piping systems were performing analyses and taking credit for components
i
to function in a manner that may not have previously been considered in the design basis.
l
l
i                  to function in a manner that may not have previously been considered in the design basis.
The engineers had not evaluated whether such reliance rnight constitute a design basis
l                  The engineers had not evaluated whether such reliance rnight constitute a design basis
change. Additionally, onsite licensee personnel performing concurrent and interrelated
                    change. Additionally, onsite licensee personnel performing concurrent and interrelated
corrective action initiatives had not been informed of the potential design engineering
                    corrective action initiatives had not been informed of the potential design engineering
.
.
                    activities that could have affected the results of these other initiatives.
activities that could have affected the results of these other initiatives.
I
I
              E3   Engineering Procedures and Documentation
E3
Engineering Procedures and Documentation
!
!
              E3.1 Review of Desian Basis and Controls for 125-Volt Direct Current (Vdc) System
E3.1
Review of Desian Basis and Controls for 125-Volt Direct Current (Vdc) System
i
a.
Inspection Scope (IP 37551)
l
i
i
              a.  Inspection Scope (IP 37551)
l
l
The inspectors reviewed the design basis document and applicable battery loading
L
calculations for the 125-Vdc system. The review was performed to ensure accuracy of
l
the documents and verify operability of the system relative to the design basis.
l
l
b.
Observations and Findinas
The 125-Vdc battery system is designed to provide service for one hour in the event of a
i
i
l                  The inspectors reviewed the design basis document and applicable battery loading
total loss of altemating current voltage at the station (station blackout). During a review
L                  calculations for the 125-Vdc system. The review was performed to ensure accuracy of
l                  the documents and verify operability of the system relative to the design basis.
l
l
of this system, the inspectors asked licensee representatives to provide any additional
!
documentation which may take into account battery loads added to the system since the
latest master calculation was generated.
l
The licensee provided the inspectors with a current listing of the master, individual
l
battery, and additional equipment calculations for the 125-Vdc system. Many of the
additional equipment loads were listed as evaluated but awaiting update to the goveming
battery calculations.
The inspectors held a meeting with the responsible system engineer to discuss the
system loads and calculations. The engineer stated to the inspectors that the process
used to review modification of loads against existing calculations did not prompt the
reviewer to consider other outstanding loads as the result of other modifications affecting
the system, to determine the cumulative effect on the 125-Vdc system. This condition
could have led to concurrent modifications not referencing appropriate updated battery
loading calculations. However, the system engineer subsequently performed
,
l
l
              b.  Observations and Findinas
conservative calculations from the modification documentation available to illustrate that
                    The 125-Vdc battery system is designed to provide service for one hour in the event of a
the 125-Vdc system was operable. The process problems identified were described in
i                  total loss of altemating current voltage at the station (station blackout). During a review
l                  of this system, the inspectors asked licensee representatives to provide any additional
!                  documentation which may take into account battery loads added to the system since the
                    latest master calculation was generated.
l                  The licensee provided the inspectors with a current listing of the master, individual
l                  battery, and additional equipment calculations for the 125-Vdc system. Many of the
                    additional equipment loads were listed as evaluated but awaiting update to the goveming
                    battery calculations.
                    The inspectors held a meeting with the responsible system engineer to discuss the
                    system loads and calculations. The engineer stated to the inspectors that the process
                    used to review modification of loads against existing calculations did not prompt the
                    reviewer to consider other outstanding loads as the result of other modifications affecting
                    the system, to determine the cumulative effect on the 125-Vdc system. This condition
                    could have led to concurrent modifications not referencing appropriate updated battery
,                  loading calculations. However, the system engineer subsequently performed
l                  conservative calculations from the modification documentation available to illustrate that
'
'
                    the 125-Vdc system was operable. The process problems identified were described in
CR 98-1528. An OD, written on April 9,1998, indicated that the system was operable.
                    CR 98-1528. An OD, written on April 9,1998, indicated that the system was operable.
The inspectors regarded the lack of maintaining accurate documentation of the 125-Vdc
                    The inspectors regarded the lack of maintaining accurate documentation of the 125-Vdc
decign basis capabilities a violation (VIO 50-266/98006-07(DRP); 50-301/98006-07(DRP))
                    decign basis capabilities a violation (VIO 50-266/98006-07(DRP); 50-301/98006-07(DRP))
of 10 CFR Part 50 Appendix B, Criterion Ill, " Design Control," which requires that design
                    of 10 CFR Part 50 Appendix B, Criterion Ill, " Design Control," which requires that design
18
                                                              18


  . .
.
            *
.
                                                                                                                      \
l    .
            changes be subject to design control measures to assure that the design basis is
            maintained. This problem dated back to about May 31,1995, when the calculations for
            the Nos.105,106, and 305 station batteries had last been updated. The inspectors
            reviewed the OD regarding the issues discussed above and had no further questions on                      )
            the matter.                                                                                              1
      c.    Conclusions                                                                                                l
l          The inspectors concluded that tne 125-Vdc system was capable of meeting design basis                      ;
                                                                                                                      '
            functions. However, the failure to maintain an up-to-date battery loading calculation was
            considered a violation of 10 CFR Part 50, Appendix B, Criteiion ill, " Design Control."
!    E3.2  Reactor Enaineerina Update of Estimated Cribcal Rate Position Calculation                                )
                                                                                                                      !
      a.   Inspection Scope (IPs 37551 and 71707)
l
l
l          The inspectors reviewed the circumstances of the suspended critical approach on
\\
*
.
changes be subject to design control measures to assure that the design basis is
maintained. This problem dated back to about May 31,1995, when the calculations for
the Nos.105,106, and 305 station batteries had last been updated. The inspectors
reviewed the OD regarding the issues discussed above and had no further questions on
)
the matter.
1
c.
Conclusions
l
The inspectors concluded that tne 125-Vdc system was capable of meeting design basis
;
functions. However, the failure to maintain an up-to-date battery loading calculation was
'
'
            March 28,1998, discussed in Section 01.1 of this report.                                                 I
considered a violation of 10 CFR Part 50, Appendix B, Criteiion ill, " Design Control."
      b.   Observations and Findinas
!
!           As discussed in Section 01.1 of this report, the first attempt to bring the Unit 2 reactor
E3.2
l           critical on March 28,1998, was suspended due to the licensse's identification during the                 3
Reactor Enaineerina Update of Estimated Cribcal Rate Position Calculation
            withdrawal of Control Bank "D" control rods that the reactor would become critical much                   !
a.
Inspection Scope (IPs 37551 and 71707)
l
l
The inspectors reviewed the circumstances of the suspended critical approach on
March 28,1998, discussed in Section 01.1 of this report.
I
'
b.
Observations and Findinas
!
As discussed in Section 01.1 of this report, the first attempt to bring the Unit 2 reactor
l
critical on March 28,1998, was suspended due to the licensse's identification during the
3
withdrawal of Control Bank "D" control rods that the reactor would become critical much
earlier than anticipated based on the estimated critical rate calculation. Operations
.
.
            earlier than anticipated based on the estimated critical rate calculation. Operations                    I
_ personnel followed appropriate procedures regarding this matter. The reactor critical rate
l          _ personnel followed appropriate procedures regarding this matter. The reactor critical rate               )
)
            position was recalculated prior to a second attempt to bring the reactor critical.
l
position was recalculated prior to a second attempt to bring the reactor critical.
i
i
l           The inspectors reviewed the information regarding the first critical approach to ascertain
l
l           why the estimated rate calculation was in error. The inspectors leamed through
The inspectors reviewed the information regarding the first critical approach to ascertain
l
why the estimated rate calculation was in error. The inspectors leamed through
!
!
interviews of reactor engineering personnel and a review of a recent reactor engineering
'
'
            interviews of reactor engineering personnel and a review of a recent reactor engineering
self-assessment, that the estimated critical rate position calculation procedure had been
            self-assessment, that the estimated critical rate position calculation procedure had been
identified as needing revision. In the self-assessment report dated December 3,1997, a
            identified as needing revision. In the self-assessment report dated December 3,1997, a
finding highlighted the need for obtaining accurate xenon information from a previous
            finding highlighted the need for obtaining accurate xenon information from a previous
shutdown to ensure the accuracy of subsequent startup critical parameters. The reactor
            shutdown to ensure the accuracy of subsequent startup critical parameters. The reactor
engineering organization had not implemented this recommendation prior to the restart of
            engineering organization had not implemented this recommendation prior to the restart of
Unit 2. The inspectors regarded this matter as another example of a problem with reactor
            Unit 2. The inspectors regarded this matter as another example of a problem with reactor
l
l           engineering performance that resulted in a previous violation
engineering performance that resulted in a previous violation
(VIO 50-266/98003-02(DRP); 50-301/98003-02(DRP)).
!
!
            (VIO 50-266/98003-02(DRP); 50-301/98003-02(DRP)).
c.
      c.    Conclusions
Conclusions
l           The inspectors concluded that the reactor engineering organization provided an
l
            inadequate critical rate position procedure to operations personnel during the startup of
The inspectors concluded that the reactor engineering organization provided an
            Unit 2. Although reactor engineering personnel had previously identified problems with
inadequate critical rate position procedure to operations personnel during the startup of
            the procedure, timely corrective actions had not been taken. The problems revealed
Unit 2. Although reactor engineering personnel had previously identified problems with
            during the startup were considered additional examples of a previously identified problem
the procedure, timely corrective actions had not been taken. The problems revealed
            with reactor engineering performance, for which a violation had been recently issued.
during the startup were considered additional examples of a previously identified problem
                                                      19
with reactor engineering performance, for which a violation had been recently issued.
?                                                                                                                     l
19
                                                                                    ---_____________________________J
?
---
J


                                                                                                              !
!
  -, .
-,
            '
.
        .
'
.
:
:
l.     E4     Engineering Staff Knowledge and Performance (IP 37551)
l.
              During a vertical slice review of the 125-Vdc system, the inspectors interviewed the
E4
              engineer responsible for the system. The discussion involved design bases and
Engineering Staff Knowledge and Performance (IP 37551)
              operability considerations for the system. The engineer had been assigned to the system         ,
During a vertical slice review of the 125-Vdc system, the inspectors interviewed the
              for less than one month.. Nevertheless, the inspectors noted that the engineer displayed         .
engineer responsible for the system. The discussion involved design bases and
              clear ownership of the 125-Vdc system and conveyed a sensitivity to emerging issues
operability considerations for the system. The engineer had been assigned to the system
              affecting the system and aggressively pursued issue resolution.                                 ;
,
        E6     Engineering Organization and Administration
for less than one month.. Nevertheless, the inspectors noted that the engineer displayed
        E6.1   Conduct of the Dutv Technical Advisor Proaram
.
          a.   Inspection Scope (IPs 37551 and 71707)
clear ownership of the 125-Vdc system and conveyed a sensitivity to emerging issues
affecting the system and aggressively pursued issue resolution.
;
E6
Engineering Organization and Administration
E6.1
Conduct of the Dutv Technical Advisor Proaram
a.
Inspection Scope (IPs 37551 and 71707)
l
l
l              As part of the monitoring of the Unit 2 reactor startup on March 28,1998, the inspectors
              reviewed the implementation of the duty technical advisor (DTA) program.
          b.  Observations and Findinas
              On the evening of March 27,1998, during the first attempt to t::ing the Unit 2 reactor
              critical, the inspectors noted that the DTA (a reactor engineer) also served as the startup
              engineer for the Unit. This individual had been the DTA for the day and was present for
,              the critical approach which began around 2:00 a.m., on March 28,1998. The DTA had
!              been called earlier in the evening to review and verify procedures and calculations for the    )
l              reactor startup. The inspectors queried the DTA as to his alertness and if he had an
              opportunity for rest earlier in the evening. The DTA indicated that he was able to get
              some brief rest and felt capable to oversee the reactor startup. The inspectors noted no
              problems regarding the DTA's performance during the subsequent startup attempt.
              The inspectors noted during the second attempt to start up Unit 2 on March 28,1998, at
              around 2:00 p.m., that the same individual was serving as the DTA (but not as the startup        i
                                                                                                                l
              engineer). The inspectors asked the DTA about the two consecutive days of work. The
              DTA indicated that due to a reduction in the number of qualified DTAs, consecutive days
l              were occasionally required.
              Concemed about the appropriateness of DTAs standing 48-hour-long watches, the
              inspectors reviewed the licensee's DTA program and response to NRC Generic
l
l
              Letter 86-04, " Policy Statement on Engineering Expertise on Shift." The inspectors noted
As part of the monitoring of the Unit 2 reactor startup on March 28,1998, the inspectors
reviewed the implementation of the duty technical advisor (DTA) program.
b.
Observations and Findinas
On the evening of March 27,1998, during the first attempt to t::ing the Unit 2 reactor
critical, the inspectors noted that the DTA (a reactor engineer) also served as the startup
engineer for the Unit. This individual had been the DTA for the day and was present for
the critical approach which began around 2:00 a.m., on March 28,1998. The DTA had
,
!
been called earlier in the evening to review and verify procedures and calculations for the
)
l
reactor startup. The inspectors queried the DTA as to his alertness and if he had an
opportunity for rest earlier in the evening. The DTA indicated that he was able to get
some brief rest and felt capable to oversee the reactor startup. The inspectors noted no
problems regarding the DTA's performance during the subsequent startup attempt.
The inspectors noted during the second attempt to start up Unit 2 on March 28,1998, at
around 2:00 p.m., that the same individual was serving as the DTA (but not as the startup
engineer). The inspectors asked the DTA about the two consecutive days of work. The
DTA indicated that due to a reduction in the number of qualified DTAs, consecutive days
l
were occasionally required.
Concemed about the appropriateness of DTAs standing 48-hour-long watches, the
inspectors reviewed the licensee's DTA program and response to NRC Generic
l
Letter 86-04, " Policy Statement on Engineering Expertise on Shift." The inspectors noted
that the program was approved by the NRC for DTAs to stand 24-hour watches and that
i
i
              that the program was approved by the NRC for DTAs to stand 24-hour watches and that
the number of available DTAs would be sufficient for adequate rotation of DTA-qualified
              the number of available DTAs would be sufficient for adequate rotation of DTA-qualified
. personnel. The inspectors also noted that the intent of the procedure describing
            . personnel. The inspectors also noted that the intent of the procedure describing
l
implementation of the DTA program (Nuclear Organization Manual Duty Technical
l
Advisor Procedure) was that DTAs would not serve a collateral position while functioning
l
l
              implementation of the DTA program (Nuclear Organization Manual Duty Technical
as a DTA. The inspectors acknowledged to station management that the DTA who
l              Advisor Procedure) was that DTAs would not serve a collateral position while functioning
served as the startup engineer for the first critical attempt was not the "on-call" reactor
l              as a DTA. The inspectors acknowledged to station management that the DTA who
engineer and that this met the verbatim requirements of the procedure However, the
              served as the startup engineer for the first critical attempt was not the "on-call" reactor
'
              engineer and that this met the verbatim requirements of the procedure However, the
fact that the DTA served as the startup engineer was not in accordance with the intent of
,
,
'
the procedure.
              fact that the DTA served as the startup engineer was not in accordance with the intent of
20
              the procedure.
                                                        20
l
l
                            _                                                                             _ _
_
_
_


r                                                                                                     1
r
  -
1
                                                                                                        !
-
    ,
i
          .                                                                                           i
.
                                                                                                        l
,
          The inspectors discussed with licensee management the concems regarding DTAs
The inspectors discussed with licensee management the concems regarding DTAs
          serving 48-hour shifts and their fitness-for-duty to fulfill their safety-related role in
serving 48-hour shifts and their fitness-for-duty to fulfill their safety-related role in
;          response to an emergency. Licensee management indicated that oversight of the                 ,
response to an emergency. Licensee management indicated that oversight of the
;
'
'
          DTA program would be assigned to the operations department manager and that                 I
,
          consecutive shifts would no longer be allowed. The operations manager issued an             '
DTA program would be assigned to the operations department manager and that
          electronic message to all DTAs regarding this matter, following the discussion with the
consecutive shifts would no longer be allowed. The operations manager issued an
          inspectors.'
'
          Licensee management also indicated that this issue would be further corrected later in
electronic message to all DTAs regarding this matter, following the discussion with the
          the year as plans were well underway to establish a shift technical advisor program which   j
inspectors.'
          would be controlled by the operations department.
Licensee management also indicated that this issue would be further corrected later in
    c.   . Conclusions
the year as plans were well underway to establish a shift technical advisor program which
          The inspectors concluded that the practice of DTAs serving two consecutive shifts
j
          (48 hours) was not consistent with the intent of program procedures and raised questions
would be controlled by the operations department.
          regarding the DTA's fitness-for-duty. Although the inspectors noted no associated           ;
c.
          performance issues, licensee management immediately revised expectations to preclude         1
. Conclusions
          potential fitness-for-duty issues.                                                           ;
The inspectors concluded that the practice of DTAs serving two consecutive shifts
                                                                                                        !
(48 hours) was not consistent with the intent of program procedures and raised questions
    E8    Miscellaneous Engineering issues
regarding the DTA's fitness-for-duty. Although the inspectors noted no associated
    E8.1   (Closed) VIO 50-266/96002-05(DRP): 50-301/96002-05(DRP): Three examples were                 !
;
          identified regarding the failure to update the FSAR as required by 10 CFR 50.71(e). The     ;
performance issues, licensee management immediately revised expectations to preclude
          licensee revised the FSAR to address the three examples and subsequently formed an         '
1
                                                                                                        j
potential fitness-for-duty issues.
          interdisciplinary process improvement team to review the FSAR update process to ensure
E8
          that all required changes were being identified and implemented in a timely manner. One
Miscellaneous Engineering issues
          outcome of the review was a revision of the FSAR change procedure (Nuclear Power
E8.1
          Business Unit Procedure, NP 5.2.6, "FSAR Updates"). However, during a followup
(Closed) VIO 50-266/96002-05(DRP): 50-301/96002-05(DRP): Three examples were
          inspection of this area (IR No. 50-266/97023(DRS); 50-301/97023(DRS)), NRC inspectors
identified regarding the failure to update the FSAR as required by 10 CFR 50.71(e). The
          identified two additional examples where the FSAR had not been revised in a timely
licensee revised the FSAR to address the three examples and subsequently formed an
          manner and a violation of 10 CFR Part 50, Appendix B, Criterion XVI, " Corrective Action,"
'j
          was cited. The earlier violation is considered closed and the corrective actions for the
interdisciplinary process improvement team to review the FSAR update process to ensure
          failure of the previous long-term corrective actions will be reviewed as part of the more
that all required changes were being identified and implemented in a timely manner. One
          recent violation (VIO 50-266/97023-03(DRS); 50-301/97023-03(DRS)).
outcome of the review was a revision of the FSAR change procedure (Nuclear Power
    E8.2   (Closed) VIO 50-266/96003-04(DRP): 50-301/96003-04(DRP): Contrary to American
Business Unit Procedure, NP 5.2.6, "FSAR Updates"). However, during a followup
          Society of Mechanical Engineers (ASME) Code post-maintenance testing requirements,
inspection of this area (IR No. 50-266/97023(DRS); 50-301/97023(DRS)), NRC inspectors
          service water pump P-32E was retumed to service in December 1995 without
identified two additional examples where the FSAR had not been revised in a timely
          determining a new vibration reference value or confirming the previous reference value.
manner and a violation of 10 CFR Part 50, Appendix B, Criterion XVI, " Corrective Action,"
          This issue involved the retum of the pump to service with vibrations in the " alert" range.
was cited. The earlier violation is considered closed and the corrective actions for the
          In a letter to the NRC dated July 19,1996, the licensee did not agree that this issue was
failure of the previous long-term corrective actions will be reviewed as part of the more
          a violation of ASME Code requirements and did not address what actions were being
recent violation (VIO 50-266/97023-03(DRS); 50-301/97023-03(DRS)).
          taken to prevent reoccurrence of a similar problem. As discussed in a letter to the
E8.2
          licensee from the NRC, dated October 30,1996, the licensee has taken steps to prevent
(Closed) VIO 50-266/96003-04(DRP): 50-301/96003-04(DRP): Contrary to American
          recurrence.
Society of Mechanical Engineers (ASME) Code post-maintenance testing requirements,
          Early in 1997, inspector review of the repair, testing, and retum-to-service of the P-32A
service water pump P-32E was retumed to service in December 1995 without
          service water pump identified that the licensee still had a misunderstanding of ASME
determining a new vibration reference value or confirming the previous reference value.
          Code reference value requirements. This misunderstanding was resolved before the
This issue involved the retum of the pump to service with vibrations in the " alert" range.
                                                    21                                               ,
In a letter to the NRC dated July 19,1996, the licensee did not agree that this issue was
                                                                                                      !
a violation of ASME Code requirements and did not address what actions were being
taken to prevent reoccurrence of a similar problem. As discussed in a letter to the
licensee from the NRC, dated October 30,1996, the licensee has taken steps to prevent
recurrence.
Early in 1997, inspector review of the repair, testing, and retum-to-service of the P-32A
service water pump identified that the licensee still had a misunderstanding of ASME
Code reference value requirements. This misunderstanding was resolved before the
21
,
!


                  _ _ _ _ _ _                                                                         .
_ _ _ _ _ _
  .
.
          -
.
    .                                                                                                   ;
-
            pump was retumed to service. Subsequent NRC review of the licensee's inservice               l
;
          testing program in mid-1997 identified no additional problems with reference value             I
.
          requirements (Section M3.1.b.4, IR No. 50-266/97010(DRS); 50-301/97010(DRS)).
pump was retumed to service. Subsequent NRC review of the licensee's inservice
    E8.3   (Closed) IFl 50-266/96006-01(DRP): 50-301/96006-01(DRP): The inspectors will review
l
          the results of the licensee's review of the inservice testing program to ensure that design
testing program in mid-1997 identified no additional problems with reference value
            basis requirements for all safety-related pumps are incorporated in IST program test         i
requirements (Section M3.1.b.4, IR No. 50-266/97010(DRS); 50-301/97010(DRS)).
            acceptance criteria. A followup programmatic review of this issue by NRC inspectors
E8.3
            (IR No. 50-266/96013(DRP); 50 301/96013(DRP)) did not identify any problems; howevel,
(Closed) IFl 50-266/96006-01(DRP): 50-301/96006-01(DRP): The inspectors will review
          the inspectors kept the IFl open pending a review of the incorporation of instrument           1
the results of the licensee's review of the inservice testing program to ensure that design
;           inaccuracies into IST acceptance criteria. In late 1996, the licensee completed               )
basis requirements for all safety-related pumps are incorporated in IST program test
i
acceptance criteria. A followup programmatic review of this issue by NRC inspectors
(IR No. 50-266/96013(DRP); 50 301/96013(DRP)) did not identify any problems; howevel,
the inspectors kept the IFl open pending a review of the incorporation of instrument
1
;
inaccuracies into IST acceptance criteria. In late 1996, the licensee completed
)
I
I
          engineering calculations addressing the incorporation of instrument inaccuracies into the     l
engineering calculations addressing the incorporation of instrument inaccuracies into the
            acceptance criteria. The inspectors reviewed Calculation No. 96-0233 for the                 '
acceptance criteria. The inspectors reviewed Calculation No. 96-0233 for the
            containment spray pumps and verified that the instrument inaccuracies had been               1
'
            incorporated into the pump IST acceptance criteria.                                           :
containment spray pumps and verified that the instrument inaccuracies had been
            Partly because of the concems identified in the past two years by the licensee and the       i
1
            NRC, the licensee initiated an extensive rebaselining of the IST program in mid-1997.       1
incorporated into the pump IST acceptance criteria.
          The rebaselining effort was being conducted by a team of two full-time contractors, one
Partly because of the concems identified in the past two years by the licensee and the
i
NRC, the licensee initiated an extensive rebaselining of the IST program in mid-1997.
1
The rebaselining effort was being conducted by a team of two full-time contractors, one
part-time contractor, and the site IST program coordinator. A brief description of the
i
i
            part-time contractor, and the site IST program coordinator. A brief description of the
rebaselining project was provided to the NRC in a letter dated December 12,1997, from
            rebaselining project was provided to the NRC in a letter dated December 12,1997, from
the licensee. To date, the project has resulted in an extensive rewriting and amplification
          the licensee. To date, the project has resulted in an extensive rewriting and amplification
of IST background documents and the generation of numerous condition reports.
            of IST background documents and the generation of numerous condition reports.                 l
E8.4
    E8.4   (Closed) LER 50-266/96016: Pressurizer Safety Valve Lift Setpoint Out of Tolerance Due
(Closed) LER 50-266/96016: Pressurizer Safety Valve Lift Setpoint Out of Tolerance Due
l
l
to Temperature Effects. This item was discussed and dispositioned in Sections E8.2
'
'
            to Temperature Effects. This item was discussed and dispositioned in Sections E8.2
and E8.3 of IR No. 50-266/98003(DRP); 50-301/98003(DRP), but the applicable LER was
            and E8.3 of IR No. 50-266/98003(DRP); 50-301/98003(DRP), but the applicable LER was
misidentified as LER 50-266/96014, which had previously been closed. This section
            misidentified as LER 50-266/96014, which had previously been closed. This section
corrects the administrative error (referencing the incorrect LER number) contained in
            corrects the administrative error (referencing the incorrect LER number) contained in
IR No. 50-266/98003(DRP); 50-301/98003(DRP).
            IR No. 50-266/98003(DRP); 50-301/98003(DRP).
E8.5 LQlosed) LER 50-266/97021: SFP Cooling System Not in Accordance With Plant Design
    E8.5 LQlosed) LER 50-266/97021: SFP Cooling System Not in Accordance With Plant Design
Basis. This item is discussed and dispositioned in Section E1.2 of this report.
,
,
            Basis. This item is discussed and dispositioned in Section E1.2 of this report.
l
l
l
l
    E8.6   (Closed) LER 50-266/97028: RWST Recirculation Piping not in Compliance with Plant
E8.6
            Design Basis. This item is discussed and dispositioned in Section E1.2 of this report.
(Closed) LER 50-266/97028: RWST Recirculation Piping not in Compliance with Plant
Design Basis. This item is discussed and dispositioned in Section E1.2 of this report.
l
l
                                              IV. Plant Support
IV. Plant Support
    R1     Radiological Protection and Chemistry (RP&C) Controls
R1
                                                                                                          '
Radiological Protection and Chemistry (RP&C) Controls
    R1.1   Unit 1 Refuelino Outaae Radiological Controls Performance Durina This inspection Period
R1.1
            (IP 71750)
Unit 1 Refuelino Outaae Radiological Controls Performance Durina This inspection Period
            The licensee had recorded 85 person-rem for the Unit 1 refueling outage at the end of the
'
            inspection period. This was on track with established goals which projected the outage
(IP 71750)
            personnel exposures to total about 130 person-rem. Personnel contamination events
The licensee had recorded 85 person-rem for the Unit 1 refueling outage at the end of the
            (PCEs) were much higher than anticipated with 81 recorded at the end of the inspection
inspection period. This was on track with established goals which projected the outage
            period. The goal for the entire outage was set at 63 PCEs. Most of the PCEs were low-
personnel exposures to total about 130 person-rem. Personnel contamination events
(PCEs) were much higher than anticipated with 81 recorded at the end of the inspection
period. The goal for the entire outage was set at 63 PCEs. Most of the PCEs were low-
l
l
1
1
                                                      22
22
                                                                                                        )
)


  - _ _ _ _ _ _ _ _ _ - _ _ _ _ _ _ _ _ _ - _ - _ _ _ - _ _ _ _ - _ _ _ _ _ _ _ _ _ _ _ _ - _ _ _ _ _ _ .
- _ _ _ _ _ _ _ _ _ - _ _ _ _ _ _ _ _ _ - _ - _ _ _ - _ _ _ _ - _ _ _ _ _ _ _ _ _ _ _ _ - _ _ _ _ _ _ .
                                          .
.
                                                                      .
.
                                                                                                          level contaminations (shoes); however, the health physics department was in the process
level contaminations (shoes); however, the health physics department was in the process
                                                                                                          of evaluating the potential causes for the higher than expected number of PCEs. The
of evaluating the potential causes for the higher than expected number of PCEs. The
                                                                                                          inspectors concluded that the licensee was maintaining good radiological controls for the
inspectors concluded that the licensee was maintaining good radiological controls for the
                                                                                                          Unit i refueling outage and an appropriate response was being undertaken to address
Unit i refueling outage and an appropriate response was being undertaken to address
                                                                                                          higher than anticipated PCEs.
higher than anticipated PCEs.
                                                                  R7                                     Quality Assurance in RP&C Activities
R7
                                                                  R7.1                                   Quality Assurance Audit of Health Physics Exit Meetina (IP 7175,0.]
Quality Assurance in RP&C Activities
                                                                                                          The inspectors attended a quality assurance department audit exit meeting on April 6,
R7.1
                                                                                                          1998. The audit included a review of various aspects of the radiation protection program
Quality Assurance Audit of Health Physics Exit Meetina (IP 7175,0.]
                                                                                                          including, instrumentation controls, offsite dose calculation manual adequacies, radiation
The inspectors attended a quality assurance department audit exit meeting on April 6,
                                                                                                          protection personnel training, and implementation of personnel dosimeter programs. The
1998. The audit included a review of various aspects of the radiation protection program
                                                                                                          auditors identified several findings within these areas which were both administrative and
including, instrumentation controls, offsite dose calculation manual adequacies, radiation
                                                                                                          performance-based. The radiation protection program manager openly discussed the
protection personnel training, and implementation of personnel dosimeter programs. The
                                                                                                          findings with the auditors to gain a clear understanding of the issues. The results of this
auditors identified several findings within these areas which were both administrative and
                                                                                                          audit will be contained in audit report A-P-98-03 which was not issued at the end of the
performance-based. The radiation protection program manager openly discussed the
                                                                                                          inspection period.
findings with the auditors to gain a clear understanding of the issues. The results of this
                                                                                                                                        V. Manaaement Meetinas
audit will be contained in audit report A-P-98-03 which was not issued at the end of the
                                                                  X1                                     Exit Meeting Summary
inspection period.
                                                                  The inspectors presented the inspection results to members of licensee management at the
V. Manaaement Meetinas
                                                                  conclusion of the inspection on April 17,1998. The licensee acknowledged the findings
X1
                                                                  presented. The inspectors asked the licensee whether any materials examined during the
Exit Meeting Summary
                                                                  inspection should be considered proprietary. No proprietary information was identified.
The inspectors presented the inspection results to members of licensee management at the
                                                                  X3                                     Meeting With Local Public Officials
conclusion of the inspection on April 17,1998. The licensee acknowledged the findings
                                                                  The inspectors, along with the Senior Resident inspector from the Kewaunee Nuclear Power
presented. The inspectors asked the licensee whether any materials examined during the
                                                                  Plant, met with local officials from the Town of Two Creeks, Kewaunee County, and Manitowoc
inspection should be considered proprietary. No proprietary information was identified.
                                                                  County on Thursday April 16,1998, at the Two Creeks Town Hall in Two Creeks, Wisconsin.
X3
                                                                  The inspectors provided the officials with an overview of NRC organizations, the resident
Meeting With Local Public Officials
                                                                  inspector program, and the inspection process. Local officials asked the inspectors questions
The inspectors, along with the Senior Resident inspector from the Kewaunee Nuclear Power
i                                                                 regarding these matters and other aspects of the NRC, which were answered by the inspectors.
Plant, met with local officials from the Town of Two Creeks, Kewaunee County, and Manitowoc
i                                                                 The officials thanked the inspectors for the opportunity to meet and ask questions.
County on Thursday April 16,1998, at the Two Creeks Town Hall in Two Creeks, Wisconsin.
The inspectors provided the officials with an overview of NRC organizations, the resident
inspector program, and the inspection process. Local officials asked the inspectors questions
i
regarding these matters and other aspects of the NRC, which were answered by the inspectors.
i
The officials thanked the inspectors for the opportunity to meet and ask questions.
l
l
l
l
l
l
l
l
                                                                                                                                                                                                                                      '
'
                                                                                                                                                    23
23
                                                                                                                                                                                                                                      ,
,
                                                                                                                                                                                      _ _ _ _ _ - _ _ _ _ _ _ - _ _ _ _ - _ _ _ _ _ -
_ _ _ _ _ - _ _ _ _ _ _ - _ _ _ _ - _ _ _ _ _ -


                                                          _ - _ _ _ _ _ _ _ _ _ _ _ _ _ - _ _ _ _ - _ _ _ _ _ _                                                   __ _ _ _ - _ _ _ _
_ - _ _ _ _ _ _ _ _ _ _ _ _ _ - _ _ _ _ - _ _ _ _ _ _
__ _ _ _ - _ _ _ _
.
.
          -
.
  .
-
                              PARTIAL LIST OF PERSONS CONTACTED
PARTIAL LIST OF PERSONS CONTACTED
  Licensee
Licensee
  Wisconsin Electric Power Company M/EPCO)
Wisconsin Electric Power Company M/EPCO)
  S. A. Patuiski, Site Vice President
S. A. Patuiski, Site Vice President
  A. J. Cavia, Plant Manager (outgoing)
A. J. Cavia, Plant Manager (outgoing)
  M. E. Reddemann, Plant Manager (incoming)
M. E. Reddemann, Plant Manager (incoming)
  R. G. Mende, Operations Manager
R. G. Mende, Operations Manager
  W. B. Fromm, Maintenance Manager
W. B. Fromm, Maintenance Manager
  J. G. Schweitzer, Site Engineering Manager
J. G. Schweitzer, Site Engineering Manager
  R. P. Farrell, Health Physics Manager
R. P. Farrell, Health Physics Manager
  D. F. Johnson, Regulatory Services and Licensing Manager
D. F. Johnson, Regulatory Services and Licensing Manager
                                                24
24
                                                                                                                _ _ _ _ - _ - _ _ - _ _ _ _ _ - _ _ _ _ _ _ _ _ _
_ _ _ _ - _ - _ _ - _ _ _ _ _ - _ _ _ _ _ _ _ _ _


  t
t
          *
*
    .
.
                                INSPECTION PROCEDURES USED
INSPECTION PROCEDURES USED
    IP 37551:   Onsite Engineering
IP 37551:
    IP 40500:   Effectiveness of Licensee Controls in identifying, Resolving, and Preventing
Onsite Engineering
                Problems
IP 40500:
    IP 61726:   Surveillance Observations
Effectiveness of Licensee Controls in identifying, Resolving, and Preventing
    IP 62707:   Maintenance Observations
Problems
    IP 71707:   Plant Operations
IP 61726:
    IP 71750:   Plant Support Activities
Surveillance Observations
    IP 92700:   Onsite Follow up of Written Reports of Noaroutine Events at Power Reactor
IP 62707:
                Facilities
Maintenance Observations
                            ITEMS OPENED, CLOSED, AND DISCUSSED
IP 71707:
    Opened
Plant Operations
    50-266/98006-01(DRP)       VIO           Failure to follow the procedure regarding reactor
IP 71750:
                                              operator observations of the main control panels
Plant Support Activities
    50-266/98006-02(DRP)       VIO           Failure to follow the procedure regarding the
IP 92700:
                                              weighing of the reactor vessel intemals lifting rig
Onsite Follow up of Written Reports of Noaroutine Events at Power Reactor
    50-301/98006-03(DRP)       NCV           Failure to perform post maintenance testing prior to
Facilities
                                              placing LTOP in service
ITEMS OPENED, CLOSED, AND DISCUSSED
    50-301/98006-04(DRP)       NCV           Failure tu implement corrective action regarding C-
Opened
                                              036
50-266/98006-01(DRP)
    50-266/98006-05(DRP)       NCV           Design control of seismically controlled piping
VIO
    50-301/98006-05(DRP)                     systems related to SFP and RWST
Failure to follow the procedure regarding reactor
    50-266/98006-06(DRP)       IFl           Followup of design basis changes to ensure
operator observations of the main control panels
    50-301/98006-06(DRP)                     proper documentation and interdepartmental
50-266/98006-02(DRP)
I                                             communications
VIO
Failure to follow the procedure regarding the
weighing of the reactor vessel intemals lifting rig
50-301/98006-03(DRP)
NCV
Failure to perform post maintenance testing prior to
placing LTOP in service
50-301/98006-04(DRP)
NCV
Failure tu implement corrective action regarding C-
036
50-266/98006-05(DRP)
NCV
Design control of seismically controlled piping
50-301/98006-05(DRP)
systems related to SFP and RWST
50-266/98006-06(DRP)
IFl
Followup of design basis changes to ensure
50-301/98006-06(DRP)
proper documentation and interdepartmental
I
communications
l
50-266/98006-07(DRP)
VIO
Failure to implement adequate design control
50-301/98006-07(DRP)
measures for 125-Vdc system calculations
i
Closed
l
l
    50-266/98006-07(DRP)        VIO            Failure to implement adequate design control
    50-301/98006-07(DRP)                      measures for 125-Vdc system calculations
i  Closed
l
l
'
'
                                                                                                                    l
50-266/98004
    50-266/98004               LER           Reactor coolant pump lube oil collection system
LER
    50-301/98004                             design nonconformance with Appendix R
Reactor coolant pump lube oil collection system
                                              Section 111.0
50-301/98004
    50-301/98002               LER           Reactor coolant pump component cooling water                         l
design nonconformance with Appendix R
                                              retum line check valve seriously degraded                             1
Section 111.0
                                                25
50-301/98002
                                                                              __________-____________-_____-______a
LER
Reactor coolant pump component cooling water
l
1
retum line check valve seriously degraded
25
__________-____________-_____-______a


  _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ - _ _ _ _ _ _ _ _ _ _ _ _ _
_ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ - _ _ _ _ _ _ _ _ _ _ _ _ _
l
l
                                                                              *
*
                                                                        .
.
                                                                                                                                                                            I
I
                                                                        50-301/95006         LER PORV post-maintenance testing not performed prior
50-301/95006
                                                                                                to establishing LTOP
LER
                                                                                                                                                                            l
PORV post-maintenance testing not performed prior
                                                                        50-301/98006-02(DRP) NCV Failure to perform post maintenance testing prior to                       i
to establishing LTOP
                                                                                                placing LTOP in service
50-301/98006-02(DRP)
                                                                        50-266/96002-01(DRP) IFl Scheduling and planning of work
NCV
                                                                        50-301/96002-01(DRP)
Failure to perform post maintenance testing prior to
                                                                        50-266/97042         LER Failure to perform containment personnel air lock
i
                                                                                                surveillance
placing LTOP in service
(                                                                       50-301/98006-03(DRP) NCV Failure to implement corrective action regarding C-
50-266/96002-01(DRP)
IFl
Scheduling and planning of work
50-301/96002-01(DRP)
50-266/97042
LER
Failure to perform containment personnel air lock
surveillance
(
50-301/98006-03(DRP)
NCV
Failure to implement corrective action regarding C-
'
'
                                                                                                036
036
                                                                        50-266/98006-04(DRP) NCV Design control of seismically controlled piping
50-266/98006-04(DRP)
                                                                        50-301/98006-04(DRP)     systems related to SFP and RWST
NCV
l                                                                       50-266/96002-05(DRP) VIO Licensees program weakness to update FSAR
Design control of seismically controlled piping
50-301/98006-04(DRP)
systems related to SFP and RWST
l
50-266/96002-05(DRP)
VIO
Licensees program weakness to update FSAR
'
'
                                                                        50-301/96002-05(DRP)
50-301/96002-05(DRP)
                                                                        50-266/%003-04(DRP) VIO IST Weakness - ASME Code                                                   I
50-266/%003-04(DRP)
                                                                        50-301/96003-04(DRP)
VIO
;                                                                       50-266/96006-01(DRP) IFl IST Program deficiencies
IST Weakness - ASME Code
l                                                                       50-301/96006-01(DRP)
50-301/96003-04(DRP)
                                                                        50-266/% 016         LER Pressurizer safety valve lift set point out of tolerance
;
                                                                                                due to temperature effects
50-266/96006-01(DRP)
                                                                        50-266/97021         LER Spent fuel pool cooling system not in accordance
IFl
j                                                                                               with plant design basis
IST Program deficiencies
l
50-301/96006-01(DRP)
50-266/% 016
LER
Pressurizer safety valve lift set point out of tolerance
due to temperature effects
50-266/97021
LER
Spent fuel pool cooling system not in accordance
j
with plant design basis
l
l
50-266/97028
LER
Refueling water storage tank recirculation piping not
l
in compliance plant design basis
Discussed
50-266/97020-02(DRP)
IFl
Evaluate procedure upgrade program
l
l
l                                                                      50-266/97028        LER Refueling water storage tank recirculation piping not
50-301/97020-02(DRP)
l                                                                                                in compliance plant design basis
                                                                        Discussed
                                                                        50-266/97020-02(DRP) IFl Evaluate procedure upgrade program
l                                                                      50-301/97020-02(DRP)
l
l
l                                                                      50-266/97006-02(DRP) IFl Review maintenance program improvements
l
l
                                                                        50-301/97066-02(DRP)
50-266/97006-02(DRP)
                                                                        50-266/97021-02(DRP) VIO Failure to test containment door interlock
IFl
                                                                        50-301/97021-02(DRP)
Review maintenance program improvements
l                                                                       50-266/97023-03(DRS) VIO Failure of corrective actions for FSAR updates
l
                                                                        50-301/97023-03(DRS)
50-301/97066-02(DRP)
                                                                                                    26
50-266/97021-02(DRP)
                                                                                                                                            _ _ _ _ _ _ _ - _ _ - _ _ _ _ -
VIO
Failure to test containment door interlock
50-301/97021-02(DRP)
l
50-266/97023-03(DRS)
VIO
Failure of corrective actions for FSAR updates
50-301/97023-03(DRS)
26
_ _ _ _ _ _ _ - _ _ - _ _ _ _
-


- - __ _ - __ _ - _ _ _ _ _ _ _______ _ ___ . _ _ - _ _ _ -                                                 _ _ _ - - . _ _ _ . _ _ - -
- - __ _ - __ _ - _ _ _ _ _ _ _______ _ ___ . _ _ - _ _ _ -
                  .                             .
_ _ _ - -
                                                                  *
. _ _ _
                                                            .
. _ _ - -
                                                                                                                                        l
.
                                                                        LIST OF ACRONYMS USED IN POINT BEACH REPORTS
.
                                                            AC     Altemating Current
*
                                                            AFW     Auxiliary Feedwater
.
                                                            ASME   American Society of Mechanical Engineers                           I
l
                                                            CCW     Component Cooling Water
LIST OF ACRONYMS USED IN POINT BEACH REPORTS
                                                            CFR     Code of Federal Regulations
AC
                                                            CLB     Current Licensing Basis
Altemating Current
                                                            CO     Control Operator
AFW
                                                            CR     Condition Report
Auxiliary Feedwater
                                                            DOS     Duty Operating Supervisor                                           j
ASME
                                                            DRP     Division of Reactor Projects
American Society of Mechanical Engineers
                                                            DTA     Duty Technical Advisors
I
                                                            ECCS   Emergency Core Cooling System
CCW
Component Cooling Water
CFR
Code of Federal Regulations
CLB
Current Licensing Basis
CO
Control Operator
CR
Condition Report
DOS
Duty Operating Supervisor
j
DRP
Division of Reactor Projects
DTA
Duty Technical Advisors
ECCS
Emergency Core Cooling System
,
,
                                                            EDG     Emergency Diesel Generator
EDG
Emergency Diesel Generator
l
l
ESF
Engineered Safety Feature
'
'
                                                            ESF    Engineered Safety Feature
EP
                                                            EP      Emergency Planning
Emergency Planning
                                                            FSAR-   Final Safety Analysis Report
FSAR-
                                                            IFl     inspection Follow-up Item
Final Safety Analysis Report
                                                            IP     Inspection Procedure
IFl
                                                            IPE     Individual Plant Evaluation
inspection Follow-up Item
l                                                           IR     inspection Report
IP
                                                            lLRT   Integrated Leak Rate Test
Inspection Procedure
                                                            IST     Inservice Testing
IPE
                                                            IT     '7 service Test Procedure
Individual Plant Evaluation
                                                            LCO     Limiting Condition for Operation
l
                                                            LER     Licensee Event Report
IR
                                                            LTOP   Low Temperature Over-Pressure Protection
inspection Report
                                                            NCV     Non-Cited Violation
lLRT
                                                            NDE     Non-Destructive Examination                                         l
Integrated Leak Rate Test
                                                            NP     Nuclear Power Business Unit Procedures                               j
IST
                                                                                                                                        '
Inservice Testing
                                                            NRC     Nuclear Regulatory Commission
IT
                                                            OD     Operability Determination
'7 service Test Procedure
                                                            01     Operating Instruction
LCO
                                                            OM     Operations Manual                                                   j
Limiting Condition for Operation
                                                            OOS     Out-of-Service                                                       i
LER
                                                                                                                                        '
Licensee Event Report
                                                            OP     Operating Procedure
LTOP
                                                            ORT     Operations Refueling Test
Low Temperature Over-Pressure Protection
                                                            PASS   Post-accident Sampling System
NCV
                                                            PCE     Personnel Contamination Event
Non-Cited Violation
                                                            POD     Prompt Operability Determination                                     '
NDE
                                                            PORV   Power-Operated Relief Valve
Non-Destructive Examination
                                                            QA     Quality Assurance
l
                                                            RCP     Reactor Coolant Pump
NP
                                                            RCS     Reactor Coolant System
Nuclear Power Business Unit Procedures
                                                            RHR     Residual Heat Removal
j
                                                            RMP     Routine Maintenance Procedure
'
                                                            RP     Radiation Protection
NRC
                                                            RV     Reactor Vessel
Nuclear Regulatory Commission
                                                            RWST   Refueling Water Storage Tank
OD
                                                                                                    27
Operability Determination
01
Operating Instruction
OM
Operations Manual
j
OOS
Out-of-Service
i
'
OP
Operating Procedure
ORT
Operations Refueling Test
PASS
Post-accident Sampling System
PCE
Personnel Contamination Event
POD
Prompt Operability Determination
'
PORV
Power-Operated Relief Valve
QA
Quality Assurance
RCP
Reactor Coolant Pump
RCS
Reactor Coolant System
RHR
Residual Heat Removal
RMP
Routine Maintenance Procedure
RP
Radiation Protection
RV
Reactor Vessel
RWST
Refueling Water Storage Tank
27


    _ - _ - _ _ - _                                                 _ - _ _ _ - - _ - _ _ - _ _ _ _ _ _ _ _ _ _ _   ___. -. -- -.
_ - _ - _ _ - _
                                                              -
_ - _ _ _ - - _ - _ _ - _ _ _ _ _ _ _ _ _ _ _
                                              .
___. -. --
                                            SE                Safety Evaluation                                                   !
-.
                                              SER               Safety Evaluation Report                                           :
.
                                                                                                                                    !
-
                                              SFP              Spent Fuel Pool                                                     '
SE
                                              SW               Service Water
Safety Evaluation
                                            TDAFW             Turbine Driven Auxiliary Feedwater
SER
                                            TS                 Technical Specification                                             )
Safety Evaluation Report
                                            T/S               Technical Specification Test
SFP
                                              URI               Unresolved item
Spent Fuel Pool
                                            Vdc               Volt Direct Current
'
                                            VIO               Violation
SW
                                              VNCR             Control Room Ventilation
Service Water
TDAFW
Turbine Driven Auxiliary Feedwater
TS
Technical Specification
)
T/S
Technical Specification Test
URI
Unresolved item
Vdc
Volt Direct Current
VIO
Violation
VNCR
Control Room Ventilation
1
1
l
l
Line 1,345: Line 1,821:
l
l
l
l
                                                                                                                  28
28
  -                 _ _ _ _ _ _ - _ _ _ _ - - _ _ _ _ _ _ _ -
-
_ _ _ _ _ _ - _ _ _ _ - - _ _ _ _ _ _ _ -


          *
*
  ,
,
l
l
  S. Patuiski                                                         -2-
S. Patuiski
                                                                                                                                          i
-2-
  The violations identified above are cited in the enclosed Notice of Violation (Notice), and the                                         j
i
  circumstances surrounding the violations are described in detailin M e enclosed report. Please
The violations identified above are cited in the enclosed Notice of Violation (Notice), and the
  note that you are required to respond to this letter and 5:iould follow the instructions specified in
j
  the enclosed Notice when preparing your response. Tns NRC will use your response, in part, to
circumstances surrounding the violations are described in detailin M e enclosed report. Please
  determine whether further enforcement action is necesnary to ensure compliance with regulatory
note that you are required to respond to this letter and 5:iould follow the instructions specified in
  requirements.
the enclosed Notice when preparing your response. Tns NRC will use your response, in part, to
  In accordance with 10 CFR 2.790 of the NRC's " Rules of Practic'.," a copy of this letter, its
determine whether further enforcement action is necesnary to ensure compliance with regulatory
  enclosures, and your response will be placed in '.he NRC Public Document Room.
requirements.
                                                                  Sir cerely,
In accordance with 10 CFR 2.790 of the NRC's " Rules of Practic'.," a copy of this letter, its
                                                                  /s/ Marc L. Dapas for
enclosures, and your response will be placed in '.he NRC Public Document Room.
                                                                  Geoffrey E. Grant, Director
Sir cerely,
                                                                  Division of Reactor Projects
/s/ Marc L. Dapas for
  Docket Nos.: 50-266, 50-301
Geoffrey E. Grant, Director
  License Nos.: DPR-24, DPR-27
Division of Reactor Projects
                                                                                                                                          l
Docket Nos.: 50-266, 50-301
  Enclosures:           1.       Notice of Violation
License Nos.: DPR-24, DPR-27
                        2.       Inspection Report
l
                                    No. 50-266/98006(DRP);
Enclosures:
                                    50-301/98006(DRP)
1.
  See Attached Distribution
Notice of Violation
  DOCUMENT NAME: G:\poin\ poi 98006.drp
2.
  To receive a copy of thle document, Indicate in the b3x "C" = Copy without attachment / enclosure "E" = Copy with attachment / enclosure
Inspection Report
  *N* = No copy
No. 50-266/98006(DRP);
    OFFICE                     Rlli                 (;-   Rlli                 (,   Rlll               ,
50-301/98006(DRP)
    NAME                       Kunowski:dp /fAL JMcBp)pfg                             Grant ///             k
See Attached Distribution
    DATE                       GM98                       N/d98                     04H95 05/05//P
DOCUMENT NAME: G:\\poin\\ poi 98006.drp
                                                                                                            '
To receive a copy of thle document, Indicate in the b3x "C" = Copy without attachment / enclosure "E" = Copy with attachment / enclosure
l                                                     OFFICIAL RECORD COPY
*N* = No copy
OFFICE
Rlli
(;-
Rlli
(,
Rlll
,
NAME
Kunowski:dp /fAL JMcBp)pfg
Grant ///
k
DATE
GM98
N/d98
04H95 05/05//P
'
l
OFFICIAL RECORD COPY
1
1
L
L


  - - - _
- - - _
              _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ - _ _ _ _ _ _ _ _ _ _ _ _ - - _ - _ _ _ _ - . - - _ _ _ . - - - _ _ _ _ _ _ - _ _ ,
_ _ _ _ _ _ _ _ _ _ _ _ _ _ _ - _ _ _ _ _ _ _ _ _ _ _ _ - - _ - _ _ _ _ - . - - _ _ _ . - - - _ _ _ _ _ _ - _ _ ,
                                                                                              .
.
!         ,
!
                      .
.
            S. Patuiski                                                                                   -3-
,
            cc w/encis:                 R. R. Grigg, President and Chief
S. Patuiski
                                            Operating Officer, WEPCO
-3-
l                                       A. J. Cayia,' Plant Manager
cc w/encis:
;                                         B. D. Burks, P.E., Director
R. R. Grigg, President and Chief
Operating Officer, WEPCO
l
A. J. Cayia,' Plant Manager
;
B. D. Burks, P.E., Director
l
l
- Bureau of Field Operations
'
'
                                          - Bureau of Field Operations
Cheryl L. Parrino, Chairman
                                        Cheryl L. Parrino, Chairman
Wisconsin Public Service
                                            Wisconsin Public Service
Commission
                                            Commission
State Liaison Officer
                                        State Liaison Officer
Distribution:
            Distribution:
CAC (E-Mail)
            CAC (E-Mail)
Project Mgr., NRR w/ encl
            Project Mgr., NRR w/ encl
A. Beati w/ encl
            A. Beati w/ encl
J. Caldwell w/ encl
            J. Caldwell w/ encl
B. Clayton w/ encl
            B. Clayton w/ encl
SRI Point Beach w/enci
            SRI Point Beach w/enci                                                                                               )
)
            DRP w/enci                                                                                                           )
DRP w/enci
            TSS w/enct
)
            DRS (2) w/encI                                                                                                       .
TSS w/enct
            Rill PRR w/enci                                                                                                       I
DRS (2) w/encI
l'           PUBLIC IE-01 wienc!
.
            Docket File w/enci                                                                                                 -
Rill PRR w/enci
            GREENS
I
            LEO (E-Mail)
l'
            DOCDESK (E-Mail)
PUBLIC IE-01 wienc!
Docket File w/enci
-
GREENS
LEO (E-Mail)
DOCDESK (E-Mail)
I
I
(
(

Latest revision as of 16:09, 16 March 2025

Insp Repts 50-266/98-06 & 50-301/98-06 on 980303-0413. Violations Noted.Major Areas Inspected:Licensee Operations, Engineering,Maint & Plant Support
ML20247D296
Person / Time
Site: Point Beach  NextEra Energy icon.png
Issue date: 05/05/1998
From:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION III)
To:
Shared Package
ML20247D285 List:
References
50-266-98-06, 50-266-98-6, 50-301-98-06, 50-301-98-6, NUDOCS 9805140331
Download: ML20247D296 (30)


See also: IR 05000266/1998006

Text

.

.

U.S. NUCLEAR REGULATORY COMMISSION

REGIONlli

Docket Nos:

50-266;50-301

Licenses No:

DPR-24; DPR-27

Report No:

50-266/98006(DRP); 50-301/98006(DRP)

Licensee:

Wisconsin Electric Power Company

Facility:

Point Beach Nuclear Power Plant, Units 1 & 2

Location:

6612 Nuclear Road

Two Rivers, WI 54241-9516

Dates:

fiarch 3 through April 13,1998

Inspectors:

F. Brown, Senior Resident inspector

P. Louden, Resident inspector

P. Simpson, Resident inspector

Approved by:

J. W. McCormick-Barger, Cliief

Reactor Projects Branch 7

9805140331 980505

PDR

ADOCK 05000266

G

PM

_ _ - _ _ _ _

.

.

9

EXECUTIVE SUMMARY

Point Beach Nuclear Plant, Units 1 & 2

NRC Inspection Report No. 50-266/98006(DRP); 50-301/98006(DRP)

This inspection includM aspects of licensee operations, engineering, maintenance, and plant

support. The report covers a six-week inspection period by the resident inspectors.

Operations

Operations personnel involved with the restart of the Unit 2 reactor exercised good

.

control of reactivity changes. Clear, consistent communications were used by operators.

(Section 01.1)

A reactor operator who was "at the controls" for a unit that was shut down and defueled,

.

left the authorized surveillance area for a short period of time without being appropriately

relieved by another reactor operator. This action was contrary to the requirements of the

licensee procedure for the conduct of operations and was a violation of Criterion V,

" Instructions, Procedures, and Drawings," of 10 CFR Part 50, Appendix B. (Section 01.2)

Operators responded appropriately when the second stage seal of an idle reactor coolant

.

pump partially opened. Planning of the pump restart and communications and procedure

adherence during the restart were appropriate and effective. (Section O2.1)

The use of tape to cover the bearing grease port of the residual heat removal pump motor

.

instead of the vendor-designed cover reflected an acceptance of substandard conditions

by auxiliary operators. (Section O2.2)

Maintenance

Main control board wire separation work was conducted in a professional and thorough

.

manner. All work observed was performed with the appropriate work order plan present

and in active use. (Section M1.1)

Maintenance and health physics organizations were not effectively prepared to perform

.

the lower intemals lift based on planning meetings conducted 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> prior to the

initiation of work. Early in the evolution, maintenance workers failed to follow procedures

resulting in a violation of Technical Specification 15.6.8.1. Laterin the evolution, the

maintenance organization displayed better control of the activity, and the lower intemals

were moved without incident. (Section M1.2)

Many observed maintenance activities were completed in accordance with requirements

.

specified in administrative and work control procedures. However, ceases were noted

where administrative requirements were not being implemented. Some of the corrective

actions for these issues were narrowly focused, and the effort to address the

inconsistencies in application of administrative requirements within the maintenance

department was not an integrated effort. (Section M1.3)

2

_ - - _ - _-_ - __-_ _ _ - __ - _- -- _ _- .

.

- _ _ _

.

j

.

.

f

.

Maintenance and operations department freeze seal pre-evolution briefings held on

.

March 17,1998, were thorough and covered command and control responsibilities,

expected communication standards, and contingencies. Teamwork between different

disciplines was evident and participants displayed a good questioning attitude.

(Section M1.5)

Enaineerina

A ventilation control panel in an emergency diesel generator room was misclassified as

.

nonsafety-related. The licensee's initial corrective actions did not include determining if

operability of the system had been challenged while the component was incorrectly

classified as being nonsafety-related. (Section E1.1)

l

The licensee identified and corrected two cases where valves between seismically

.

l

qualified piping systems and non-qualified piping systems were not maintained in a

I

closed position as required by the Final Safety Analysis Report. (Section E1.2)

!

Offsite, corporate office-based engineering personnel working on a corrective action

.

commitment initiative to assess the adequacy of a separation of seismically qualified and

!

non-qualified piping systems were performing analyses and taking credit for components

to function in a manner that may not have previously been considered in the design basis.

The engineers had not evaluated whether such reliance might constitute a design basis

j

change. Additionally, onsite licensee personnel performing concurrent and interrelated

corrective action initiatives had not been informed of the potential design engineering

activities that could have affected the results of these other initiatives. (Section E1.3)

The inspectors concluded that the 125-Volt direct current (Vde) system was capable of

.

l

meeting design basis functions. However, the failure to maintain an up-to-date battery

loading calculation was considered a violation of 10 CFR Part 50, Appendix B,

Criterion Ill, " Design Control." (Section E3.1)

The reactor engineering organization did not provide accurate critical rats position data to

.

l

operations personnel during an initial attempt to startup Unit 2. The problems revealed

'

during the startup were considered additional examples of reactor engineering

performance concems which were the subject of a Notice of Violation from Inspection

l

Report No. 50-266/98003(DRP); 50-301/98003(DRP). (Section E3.2)

l

The practice of duty technical advisors (DTAs) serving two consecutive 24-hour watches

.

was not consistent with the intent of program procedures and raised questions regarding

the DTA's fitness-for-duty. Although, no specific performance issues were identified as a

result of the DTA standing consecutive watches, licensee management immediately

revised expectations regarding this practice to preclude potential fitness-for-duty issues.

(Section E6.1)

l

1

I

I

l

3

l

L_________-------__---__---._---------__

, - _ _ _ - _ _ - _ _ _ _ _ - _ _ - - _ _ - _ _ _

_ - -

-

_ _ _

-

.

.

Plant Support

Perronnel exposures during the Unit i refueling outage were meeting established

.

.

licensee goals. The number of personnel contamination events was higher than

l

anticipated; however, most of the events were minor shoe contaminations. The health

physics manager initiated a review of the causes for the higher than anticipated number

of personnel contamination events. None of the events resulted in significant exposure of

!

personnel. (Section R1.1)

l

I

1

l

l

'

l

f

I

l

i

4

I

!

1

_ _ _ . _

._ _ _ _ _ _ _ _ _ _ _ _ _ _ - _ _ _ _ _ _ _ _ _ - - -

._ _

. _ _ _ _

_

.

.

.

.

i

Report Details

Summary of Plant Status

During this inspection period, Unit 1 was shutdown in a continuation of the Cycle 24 refueling

outage. ' Unit 2 was shutdown on March 5,1998, in accordance with Technical Specification

(T/S) 15.3.0., because the compenent cooling water (CCW) system was declared inoperable.

Detailed engineering analysis subsequently determined that the CCW system was operable.-

Unit 2 was restarted on March 28,1998, and operated at 100 percent power for the remainder of

the inspection period.

Inspection Focus

l

j

During this inspection period, the inspectors focused on conduct of plant operations, continued a

vertical slice review of the 125-volt direct current (Vde) system, and completed routine inspection

activities.

l

1. Operations

01

Conduct of Operations

l

01.1

Unit 2 Reactor Startuo (Inspection Procedure (IP) 71707)

During the restart of the Unit 2 reactor on March 28,1998, problems encountered during

the attempt to make the reactor critical resulted in the licensee suspending the criticality

l

attempt. The reactor was made critical later the same day following a review of the

earlier problems and a recalculation of the estimated critical rate position. Problems

associated with the initial estimated critical rate position calculation are discussed in

Section E3.2 of this report. Operations personnelinvolved with the restart of the Unit 2

reactor exercised good command and control of reactivity changes and used clear,

consistent three-way communications.

01.2 Unit Operator Left the Authorized "At the Controls" Area

a.

Inspection Scope (IP 71707)

The inspectors reviewed the circumstances regarding the failure of an onshift reactor

operator (control operator (CO)) to remain within authorized surveillance areas in the

control room.

l

l

b.

Observations and Findingg

'

,

The inspectors were in the control room monitoring a Unit 2 non-routine activity on

March 14,1998. At approximately 9:00 p.m., the inspectors noted that the Unit 1 CO was

l

not in an authorized surveillance area for Unit 1, which was defueled at the time. Shortly

i.

thereafter, the Unit 1 CO reentered the authorized surveillance area from the control room

back panel area. The CO was absent from the authorized area for about one minute.

The T/S minimem manning requirements were satisfied during the CO's absence;

i

however, Operations Manual (OM) 1.1, " Conduct of Plant Operations," Revision 1,

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Attachment 2, Paragraph 2.3, required the reactor operator "at the controls" to remain in

the authorized area unless relieved. The inspectors discussed the CO's absence from

the authorized area with the duty operating supervisor (DOS, a senior reactor operator).

The DOS stated that the CO had been released from the authorized area for a short

period of time, and that this was acceptable because Unit 1 was defueled. The

inspectors pointed out that OM1.1 allowed no exceptions. This issue was further

discussed with the operations manager, who acknowledged that OM 1.1 required the unit

CO to remain in the authorized area under all fuel loading conditions. The failure of the

Unit 1 CO to remain in the authorized area was a violation (VIO 50-266/98006-01(DRP))

of 10 CFR Part 50, Appendix B, Criterion V, " Instructions, Procedures, and Drawings,"

which requires that activities affecting quality be performed in accordance with

procedures. Condition Report (CR) 98-1075 was written to document this event, and the

operations manager sent all operators an electronic memorandum which reiterated the

requirements of OM 1.1 for an operator "at the controls."

The inspectors also identified a discrepancy in OM 1.1. Figure 1 and Section 2.8 of

Attachment 1 differed concoming the control room area the DOS was to occupy. The

licensee's practice was to allow the DOS to sit on a raised platform in the control room,

which was consistent with Section 2.8 but was not allowed by Figure 1. The inspectors

identified the discrepancy to the duty shift superintendent (DSS, a senior reactor

operator). The DSS stated the discrepancy had already been identified by operations

personnel via the procedure change process about six months earlier but was not yet

corrected. The DSS wrote a CR to document the discrepancy on March 19,1998. This

discrepancy was corrected the same day with a temporary procedure change.

During this inspection period, the inspectors noted that the operations department had a

significant number of outstanding procedure change requests and was in the process of

upgrading operations procedures. Licensee management indicated that priorities were

set to accomplish the procedure upgrade work within existing resource constraints. The

correction of OM 1.1, identified six months earlier by operators, was not high in the

priority scheme. The inspectors commented to operations management that procedural

adherence and operator identification of needed procedure changes may be adversely

affected given the large backlog which impacted the timeliness of processing procedure

changes. However, the inspectors noted that progress was being made in upgrading

operations department procedures overall.

c.

Conclusions

The inspectors concluded that the CO who left the "at the controls" area for a bnef time

on March 14,1998, without obtaining an appropriate relief, was not performing duties in

accordance with OM 1.1. This was considered a violation of 10 CFR Part 50,

Appendix B. The inspectors also identified a discrepancy in OM 1.1, which the licensee

subsequently corrected. The procedure upgrade program contained a substantial

backlog of identified changes that needed to be made; however, a prioritization list was

being followed and some progress was being made.

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02

Operational Status of Facilities and Equipment

O2.1

Reactor Coolant Pumo (RCP) Seal Leakaae

a.

(nspection Scope (IP 71707)

The inspectors reviewed the licensee's response to excessive leakage from the

Unit 2 "B" RCP (2P-1B) second stage seal.

b.

Observations and Findings

On March 10,1998, operators noted excessive flow through the second stage seal of

RCP 2P-1B. Unit 2 was in cold shutdown and reactor coolant pressure was 300 pounds

per square inch gauge (psig) with the "A" RCP (2P-1 A) operating and the "B" RCP (2P-

1B) idle. Upon the discovery of the excessive seal leakage, the operating crew entered

Abnormal Operating Procedure 18. "RCP Malfunction," Revision 8. In accordance with

i

that procedure, pump 2P-1 A was secured, the reactor was depressurized to about

i

50 psig, and tne RCP seal water retum valves were closed. These actions terminated

,

the excessive flow. The inspectors noted thet the operating crew referenced the

j

appropriate T/S for reactor coolant system leakage. The licensee wrote a condition report

I

to document the event.

l

The licensee formed a multi-disciplinary team to assess the condition of the 2P-1B seal

package and concluded that the second stage seal had partially opened, but had not

failed. A temporary change was made to Operating Procedure (OP) 3C, " Hot Shutdown

1

to Cold Shutdown," Revision 69, to provide instructions for starting 2P-1B to allow for

further evaluation of the seal's condition. The inspectors reviewed the change to OP 3C

and the referenced sections of OP 4B, "RCP Operation," Revision 34, and concluded that

the changes were appropriate for the circumstances. An operating crew started

RCP 2P-1B without incident on March 14,1998. The second stage seal reseated during

the pump start. The inspectors observed appropriate and effective communications,

planning, and performance of pump start activities in the control room during this

evolution.

c.

Conclusions

Operators responded appropriately when the second stage seal of an idle RCP partially

l

opened. Planning of the pump restart and communications and procedure adherence

during the restart were appropriate and effective.

O2.2 Residual Heat Removal (RHR) Pump Motor Grease (IP 71707)

i

During a routine walkdown of safety-related systems, the inspectors identified a

,

discrepancy in the amount of grease present on the outboard bearings of the

l

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four RHR pump motors. The amount ranged from grease fully covering the bearings to

being hardly visible. The inspectors also noted that tape was used to cover the

Unit 1 RHR "A" pump motor outboard bearing grease port in lieu of the vendor-designed

i

cover. When notified of the findings, the component engineers investigated the situation

and informally determined that the pumps were still operable. Operations personnel

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wrote a condition report regarding the matter and requested a formal operability

I

determination (OD). The licensee concluded in the OD that the pumps remained

operable.

1

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The inspectors concluded that the bearing grease levels were not an operability concem.

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However, the use of tape to cover the bearing grease port of the safety-related

RHR pump instead of the vendor-designed cover reflected auxiliary operator acceptance

of substandard conditions.

O3

Operations Procedures and Documentation

O3.1

Update on Station Wide Procedure Uparade Proaram (IPs 71707. 62707. and 37551)

In a previous inspection report (No. 50-266/97020(DRP); 50-301/97020(DRP)), the

inspectors opened an inspection follow up item (IFI) to evaluate the licensee's ongoing

procedure upgrade program and verify that:

j

upper tier administrative procedures for procedure adherence and procedural

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control of activities were consistent wia the current licensing basis and NRC

guidance,

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the methods for establishing procedural controis were commensurate with

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licensee staff training and supervisory oversight such that activities affecting

i

safety were performed in a controlled manner and with predictable results, and

the licensee's process for assuring that work plans were not inappropriately used

+

to circumvent procedural change requirements were adequate.

]

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Over the past six months, the inspectors have identified several instances where

procedural controls were either inadequate for the circumstances or were not adhered to

l

by licensee personnel. Sections 01.2, M1.2, M1.3, and E3.2 of this report discuss other

i

examples of procedural problems still evident at the station.

.

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Notwithstanding these problems, the inspectors have noted an increased sensitivity to

procedural quality issues and some progress in upgrading procedures. Additionally,

insufficient time has passed to determine the effect of the licensee' procedure upgrade

project. Therefore, the inspectors will leave IFl 50-266/97020-02(DRP);

50-301/97020-02(DRP) open for an additional six-month period to track the programmatic

aspects of procedure content, use, and adherence.

07

Quality Assurance in Operations

07.1 Operations Quality Assurance Audii(IP 71707)

The inspectors attended a quality assurance department audit exit on March 13,1998.

The audit focused on operations department administrative controls and operator

4

performance. The meeting was well attended by operations department personnel and

plant management. Operations management was receptive to the auditors' findings. The

inspectors noted that most of the findings from the audit were more administrative in

nature rather than performance-based. The inspectors subsequently reviewed the issued

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audit report (No. A-P-98-03) and verified that the issues discussed at the exit meeting

were consistent with those documented in the report.

1

08

Miscellaneous Operations issues

08.1

(Closed) Licensee Event Report (LER) 50-266/98004: 50-301/98004: Resc.or coolant

pump lube oil collection system design nonconformance with Appendix R, Section 111.0.

1'

This issue was discussed and dispositioned in accordance with the NRC Enforcement

Policy in inspection Report No. 50-266/98003(DRP); 50-301/98003(DRP), Section O2.1.

No further action is necessary regarding this matter.

08.2 (Closed) LER 50-301/98002: Reactor coolant pump component cooling water retum line

I

check valve found seriously degraded. The CCW system containment retum check

valve (2CC-745) was radiographer and found in the open position. This valve provides a

redundant means for preventing loss of CCW fluid in the event of a failure of a CCW pipe

j

inside the containment. The licensee rebuilt the intamals of the valve and the repairs

!

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were deemed to be adequate. The inspectors had no further questions regarding this

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matter.

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II. Mainte_n_ance

M1

Conduct of Maintenance

M1.1 Main Control Board Wire Separation Maintenance Activities

[nLspection Scope (IP 62707)

a.

r

The inspectors observed and reviewed the following maintenance activities which were

part of the corrective actions to resolve discrepancies between redundant safety-relsted

equipment:

Work Order Plan 9705320, " Sleeve / Wrap Cables For Circuit 1 A-06 Bus

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Voltmeter," and

Work Order Plan 9705324, " Sleeve / Wrap Cables For Circuit Supply

.

Breaker 1 A52-77 to Bus 1 A-04."

The planned activities included separating and sleeving electrical wires in some control

room panels associated with control and indication circuits for the Class 1E electrical

buses and power sources,

b.

Observations and Findinos

The scope of the planned cable separation work required entry into the T/S 15.3.7.B.1.g.

limiting condition for operation (LCO) for Unit 2 (Unit 1 was defueled at the time) since the

' B" train of the 4.16-kilovolt bus safeguards switchgear (Bus 1 A-06) did not have its

emergency power source available because of the protective tagout boundary. The

inspectors verified that the appropriate T/S LCOs had been entered for the plant

conditions and scope of planued work.

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The inspectors noted good coordination and communication between the work control

center, control room, and maintenance personnel. The job supervisor briefed the control

room personnel on the specifics of each work order plan and walked through each

package with the maintenance crew doing the work. Quality control personnel were

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present whenever required by the work order plans and quality control hold points were

properly verified and signed off.

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The maintenance crews used self-verification checks in the cramped and sensitive work

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environment. Workers also displayed good questioning attitudes during the course of the

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work. Worker-identified discrepancies in work plans were called to the attention of

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maintenance supervision and corrected appropriately.

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c.

Conclusions

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The inspectors concluded that the control board wire separation work was performed in a

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professional and thorough manner, All work observed was performed with the

appropriate work order plan present and being appropriately referenced.

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M1.2 Unit 1 Reactor Vessel Lower intemals Lift

a.

Inspection Scope (IP 62707)

The inspectors observed the planning and execution of the Unit i reactor vessel (RV)

i

lower intemals lift.

b.

Obser<ations and Findinas -

The inspectors attended a work preparation briefing on March 3,1998, which was held to

discuss the various aspects of the lower intamals lifting evolution. Work group

l

responsibilities were identified and Routine Maintenance Procedure (RMP) 9053, "RV

Intemals Removal and Installation," Revision 1, was reviewed. Health physics

,

considerations were discussed; however, radiation work permits had not been completed.

'

The inspectors made the following observations regarding the briefing:

Contrary to Nuclear Procedure 1.2.6, " Infrequently Performed Tests and

.

Evolutions," Revision 4, the work activity was not categorized as an infrequently

performed test or evolution. This condition was subsequently corrected prior to

the beginning of work.

Health physics information discussed was not complete nor fully evaluated prior

.

to the planning meeting. For example, the radiation work permits had not been

prepared.

l

Overall, discussions at the briefing (held 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> before the initiation of work)

.

indicated that many aspects of the job had not been thoroughly evaluated.

The initial attempt to lift the lower intemals was performed under the direction of a

maintenance supervisor. A senior manager was present in the containment to provide

oversight. The inspectors observed that the maintenance crew attached the containment

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polar crane hook to the "intemals lift rig," a special lifting platform, without inserting a load

cell between the hook and lift rig, as required by Step 7.3.7.f. of the RMP. The purpose

of the load cell was to provide early indication of binding during crane load vertical

movement. The inspectors asked the maintenance supervisor why this step had not

been completed. The supervisor stated that the lift rig was to be moved to the other side

of the containment and the load cell would then be installed. This action would have

been acceptable, since the procedure specifically only prevented the lifting rig from being

positioned above the reactor vessel without the installed load cell. However, the crew

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proceeded with positioning the lift rig above the RV with the intent of lowering the lift rig

into place on the RV and then installing the load cell. Positioning the intemals lift rig

above the reactor vessel without the load cell installed was a violation

(VIO 50-266/98006-02(DRP)) of T/S 15.6.81 for failure to follow procedures. Prior to the

lift rig being lowered onto the RV, the senior manager in containment recognized that the

procedural requirements were being violated and stopped work. The action was

documented on CR 98-0831. A temporary change was made to RMP 9053 to allow

installation of the load cell after the lift rig was landed on the RV While the procedure

change was being processed, involved maintenance personnel stated that the original

procedure had been ir;dequate. The inspectors concluded that the steps in the original

procedure could have been performed as written. Additionally, the inspectors noted that

maintenance staff had ample opportunity during the pre-job briefing to decide how to

perform the steps as written or to identify attemate ways to perform the lift, and make any

,

necessary procedural changes.

The maintenance crew attempted to lower the lift rig onto the RV after the temporary

change was processed for the RMP. The three guide bushings on the lift rig were not

proper 1y aligned with the three guide studs in the RV flange, and at least one bushing was

observed to be resting on the corresponding guide tube. The full weight of the lift rig

appeared to be placed on the guide bushings which were resting on top of the guide

studs. The crane operator could not quickly identify the misalignment because the load

cell was not present to indicate reduced weight on the crane as the crane hook was

lowered. The lift rig was raised off the guide studs and rotated into proper alignment. On

the second attempt at lowering the !ift rig, the mounting plates for two of the guide

bushings were found to have been knocked out of alignment to the extent that the guide

bushings would no longer slide down the guide studs. The lift rig was transferred back to

a laydown area, and the guide bushing mounting plates were realigned. Lifting

operations were suspended to allow for a shift change of personnel.

A pre-job briefing was conducted for the on-coming shift personnel. Overall, the briefing

was conducted well. The maintenance supervisor in charge of the evolution displayed a

clear understanding of the task and clearly outlined roles and responsibilities of the work

,

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crew members. During the conduct of the intemals lift, the maintenance supervisor

maintained a " big picture" oversight of the activity. Having noted the procedural

compliance problems during the previous shift, the work crew leader was deliberate in

taking actions and frequently referenced the RMP to ensure steps were appropriately

completed. The lift was conducted very methodically and was controlled well. The lower

intemals were placed in the storage area of the Unit 1 cavity area without incident.

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c.

Conclusions

The inspectors concluded that the maintenance and health physics organizations were

not adequately prepared to perform the lower intemals lift based on planning meetings

conducted 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> prior to the initiation of work. In addition, early in the evolution, the

inspectors identified a failure of maintenance workers to follow procedures as required by

T/S. This was considered a violation. Later in the evolution, the maintenance

organization displayed better control of the activity and the lower internals were moved

without incident.

M1.3 Inconsistent Application of Administrative Controls in Maintenance

a.

Inspection Scope (IPs 62707 and 40500)

The inspectors assessed the maintenance department's implementation of administrative

controls, including procedure adherence.

b.

Observations and Findinas

Maintenance personnel were observed to be performing many maintenance activities in

full compliance with procedural and other administrative controls. However, the failure to

utilize the procedural controls in place during the lower intemals lift, and the failure to

effectively utilize the pre-job brief to ensure the appropriateness of the planned method of

)

performing work during the lower intemals lift, described in Section M1.2 above, were

indicative of inconsistencies in the maintenance department's application of standard

administrative controls. The inspectors identified two other minor discrepancies in the

application of administrative controls by the maintenance department during this period.

These conditions were discussed with licensee staff and were corrected under

CR 98-0917 and CR 98-1168. Additional,' unrelated examples of inconsistent application

of administrative controls were identified by the licensee, and were documented in

CR 98-1369 ar~i CR 98-1463. Similar issues were discussed in Section M2.2 of

IR No. 50-266i98003(DRP); 50-301/98003(DRP).

l

Specific corrective actions were taken for each identified discrepancy, but the inspectors

noted that there was no broad-based initiative to address the observed discrepancies.

j

Additionally, some of the corrective actions were narrowly focused. For instance, the only

corrective action documented for the RV lower intemals lift procedure violation

(CR 98-0831) was a permanent change to the procedure to add greater flexibility in the

performance of work steps. This did not appear to address all of the performance issues

discussed in Section M1.2 above. This concem was discussed with the maintenance

manager, who indicated that the performance discrepancies were not pervasive, and that

.

various initiatives were in place to improve the performance of maintenance activities.

i

The maintenance manager further stated that a coordinated effort to address both long-

!.

term corrective actions and interim actions within the department was worth

consideration.

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c.

Conclusions

Many of the maintenance activities observed were completed in accordance with

requirements specified in administrative and work control procedures. However, the

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inspectors noted cases where administrative requirements were not being implemented.

l

The licensee's corrective action program also identified similar examples of this problem.

Some of the corrective actions for these issues were narrowly focused and lacked an

integrated effort to address the inconsistencies in application of administrative controls

i

within the maintenance department.

M1.4 Troubleshooting a Breaker Indication Failure

l

The inspectors reviewed the licensee's troubleshooting and corrective actions for a failure

of the control room indication for motor-driven auxiliary feedwater pump P-38A. The

associated work order Packages 9708867 and 9804735 were complete and thorough.

No administrative or technical concems were identified.

M1.5 Freeze Seal for Repair of Component Coolina Water Check Valve. 2CC-745 (IP 61707)

The licensee used a freeze seal to assist in the performance of a visual inspection and

repair of 2CC-745. The inspectors verified that the licensee had taken appropriate

measures to address industry-related problems with freeze seals. Maintenance

Procedure RMP 9327, "CC-745 Swing Check Vane Inspection," Revision 0, and

10 CFR 50.59 safety evaluation (SE)98-037 contained requirements that reflected these

l

measures and were determined to be adequate by the inspectors.

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The inspectors attended the maintenance and operations department freeze seal pre-

evolution briefings held on March 17,1998. The briefings were thorough and covered

command and control responsibilities, expected communication standards, and

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contingencies. Teamwork between the different disciplines was evident and participants

i

displayed a good questioning attitude. The licensee completed inspection and repair of

!

2CC-745 as planned.

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M8

Miscellaneous Maintenance issues

M8.1 (Closed) LER 50-301/95006: PORV (Power-Operated Relief Valve) Post-Maintenance

l

Testing Not Performed Prior to Establishing LTOP (Low Temperature Over-Pressure

l

Protection). The licensee identified that LTOP was not properly established after the

i

reactor vessel head was reinstalled because one of two PORVs required for LTOP was

inoperable. The valve was considered inoperable because post-maintenance testing had

not been completed. A root cause evaluation by the licensee identified that a

l

misunderstanding in the work control center resulted in the post-maintenance test for the

l

valve not being performed before the reactor head was reinstalled. With the reactor head

installed, LTOP was required. In addition, control room operators were unaware that the

l

post-maintenance test had not been completed.

Two operable PORVs were required for LTOP, but the T/S allowed one valve to be

!

inoperable for a limited time period. The licensee was allowed 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> to restore the

!

inoperable PORV and an additional 8 hours9.259259e-5 days <br />0.00222 hours <br />1.322751e-5 weeks <br />3.044e-6 months <br /> to depressurize and vent the reactor coolant

system if the PORV could not be made operable. However, the valve was inoperable for

about 34 hours3.935185e-4 days <br />0.00944 hours <br />5.621693e-5 weeks <br />1.2937e-5 months <br /> and the reactor coolant system had not been depressurized or vented.

Licensee management counseled operators and work control center staff on the

inappropriate delay in completing the post-maintenance test and revised several

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procedures to highlight the need for PORV operability (and establishing LTOP) prior to

reactor head installation. The problem has not reoccurred and an extensive review of the

post-maintenance testing process by the licensee in the past year, with concurrent NRC

monitoring of that review (see, for example, Sections M1.1 and M3.1 of

IR No. 50-266/97010(DRS); 50-301/97010(DRS), has given further assurance that this

will remain an isolated event. This licensee-identified and corrected violation is being

treated as a non-cited violation (NCV 50-301/98006-03(DRP)), consistent with

Section Vll.B.1 of the NRC Enforcement Policy.

M8.2 (Closed) IFl 50-266/%002-01(DRP): 50-301/96002-01(DRP): This IFl comprised several

inspector concems generally related to work planning and scheduling. One of those

concems was that an SE which addressed equipment operability could be prepared and

approved without control room personnel being made aware of possible changes to the

operability status of plant equipment specified in the SE. Because of this and other

problems with the SE process, the licensee reviewed numerous existing SEs, extensively

l

restructured the goveming procedure for conducting an SE, trained plant staff on the

revised procedure, and established a multi-disciplinary team of which a member would

review all SE screenings. Recent NRC inspections (irs No. 50-266/97010(DRS);

50-301/97010(DRS) and No. 50-266/97023(DRS); 50-301/97023(DRS)) have identified

that the SE process has improved. The original concem of this IFl has been adequately

addressed.

A second concem pertained to the concurrent use of a CCW pump as the redundam

pump for two other CCW pumps. This concem was adequately addressed with the

revision (in June 1997) of T/S 15.3.3.C. for the CCW pumps. This revision removed the

previous ambiguity on redundant pumps and does not allow the use of a CCW pump

assigned to one Unit as a redundant pump for the other Unit.

,

The remaining two items pertained specifically to poor planning and scheduling of work

'

on an emergency diesel generator (EDG) and a CCW pump. Recent inspection reports

(irs No. 50-266/97003(DRP); 50-301/97003(DRP), No. 50-266/97006(DRP);

50-301/97006(DRP), No. 50-266/97013(DRP); 50-301/97013(DRP), and

No. 50-266/97021(DRP); 50-301/97021(DRP)) document additionalinstances of poor

work planning and scheduling. Although none of these items involved violations of NRC

requirements, they indicated that the work planning and scheduling process was weak

As discussed in IR No. 50-266/97006(DRP); 50-301/97006(DRP), the licensee has

recently undertaken several initiatives following an extensive maintenance program

improvement review. Because the implementation of these programmatic initiatives is

being tracked as an IFl (50-266/97006-02(DRP); 50-301/97006-02(DRP)) and the original

SE and CCW concems discussed above have been adequately addressed, the two

concerns about specific work planning and scheduling problems are considered closed.

M8.3 (Closed) LER 50-266/97042: Failure to perform containment personnel air lock

surveillance while door interlock is inoperable. The events and circumstances of this LER

were discussed in IR No. 50-266/97021(DRP); 50-301/97021(DRP), Section M2.1. A

Notice of Violation was issued regarding this matter. Therefore, this LFR is considered

l

closed with the existing open violation (VIO 50-266/97021-02(DRP);

i

50-301/97021-02(DRP)) serving as the inspection tracking mechanism for completion of

the corrective actions.

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lil. Enaineerina

E1

Conduct of Engineering

E1.1

EDG Room Ventilation System Safety Classification

a.

Inspection Scope UP 37551)

The inspectors reviewed aspects of the safety classification of the EDG room ventilation

systems.

b.

Observations and Findinas

The inspectors reviewed the safety classification of the G-01 and G-02 EDG room

ventilation system components. This review was performed while independently

assessing the technical merits of an OD associated with EDG output ratings at elevated

room temperatures. The inspectors noted that the G-01 exhaust fan control panel

(C-032) was classified as safety-related; however, the G-02 exhaust fan control panel

(C-036) was classified as nonsafety-related. The inspectors questioned the system

engineer about this difference. After reviewing the component history, the system

engineer determined that the list of safety-related components had not been appropriately

updated to add C-036 as committed to in LER 50-301/91001-01. This problem was

documented in CR 98-1084.

The inspectors reviewcd the corrective actions for CR 98-1084 to ensure that the issue

had been adequately addressed. The corrective actions consisted of a broad review of

the EDG room ventilation system to determine whether any other discrepancies existed,

and a review to determine whether the condition was reportable. While these two

corrective actions were appropriate, both the CR and the corrective action documents

specified that the as-found condition was administrative in nature. The problem could

have been more substantial had the appropriate configuration and material controls not

been maintained between the time C-036 was dedicated as being safety-related and the

identification of the error. The inspectors communicated this concem to the appropriate

system engineering supervisor, who initiated an additional corrective action to review the

maintenance and modification history of C-036 to ensure that its configuration and

material status had not been compromised. No problems were identified during this

review.

1

The inspectors considered the safety significance of this specific issue to be minor;

therefore, the failure to implement effective corrective actions regarding the safety

classification of C-036 (with respect to LER 50-301/91001-01 and CR 98-1084) was a

. non-cited violation (NCV 50-301/98006-04) of 10 CFR Part 50, Appendix B, Criterion XVI,

" Corrective Action," consistent with Section IV of the NRC Enforcement Policy.

c.

Conclusions

The inspectors identified a minor discrepancy in the licensee's list of safety-related

components. Specifically, a ventilation control panel in an EDG room was misclassified.

The licensee's initial corrective actions did not include determining if the ventilation

system operability had been challenged while the component was incorrectly classified as

15

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.

.

.

being nonsafety-related. Subsequent review indicated no problems in this area and the

discrepancy was corrected.

E1.2

Seismic Isolation in Pipina Systems

a.

Inspection Scope (IP 92700)

The inspectors reviewed two LERs that dealt with discrepancies conceming the

conformance of plant piping systems to Final Safety Analysis Report (FSAR)

commitments.

b.

Observations and Findinas

Licensee Event Report 50-266/97021 documented the failure to maintain two valves in

the spent fuel pool (SFP) cooling system in a normally closed position. These two valves

separated seismically qualified portions of the SFP cooling system from non-seismically

qualified portions of the system. Licensee Event Report 50-266/97028 documented that

piping which was not seismically qualified was connected to the seismically qualified

refueling water storage tank (RWST) by way of normally open valves. The FSAR requires

that valves which separate seismically qualified from non-seismically qualified systems be

normally closed.

The licensee initiated a broad assessment of a!I systems which contained a seismically

qualified to non-qualified interface. Corrective actions were planned for all pipe systems

where adequate system separation did not exist. These actions were discussed with the

j

NRC during public meetings and were documented in docketed letters to the NRC dated

July 25,1997 (NPL 97-0432), and December 19,1997 (NPL 97-0803). The inspectors

reviewed the documentation associated with this issue and considered the docketed

information to be accurate and comprehensive. The corrective actions were considered

to be appropriate. This licensee-identified and corrected, non-repetitive failure to

maintain the SFP cooling system and RWST recirculation pipe isolation valves in the

design position (normally closed), was a non-cited violation (NCV 50-266/98006-05(DRP);

50-301/98006-05(DRP)) of 10 CFR Part 50, Appendix B, Criterion lil, " Design Control,"

cor.sistent with Section Vll.B.1 of the NRC Enforcement Policy,

C_ nclusions

o

c.

The licensee identified and implemented effective corrective actions for two cases where

valves between seismically qualified piping systems and non-qualified piping systems

were not maintained in a closed position as required by the FSAR.

E1.3

Maintaining Desian Basis Inteority

l

a.

Inspection Scope (IP 37551)

l

l

The inspectors reviewed the current status of licensee actions to ensure conformance of

plant piping systems to FSAR commitments.

16

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,

,

a

j

b.

Observations and Findinas

)

The inspectors discussed the status of the licensee's ongoing assessments of the

adequacy of the separation of seismically qualified and non-qualified piping systems with

the cognizant design engineering personnel. The engineers described the screening

process being used to determine whether various systems were in conformance with the

FSAR commitments, and whether modifications would be required for systems and

components which were operable, but not in compliance with the existing FSAR. The

screening criteria included the identification of motor-operated valves and check valves

which could serve the function of a normally closed valva. When such motor-operated

valves or check valves existed, additional corrective actions for those systems were not

considered necessary to address the seismically qualified to non-qualified separation

concem. However, the criteria did not require the evaluation of whether such motor-

operated valves or check valves were considered seismic-class boundsry valves in the

system design and licensing bases.

The inspectors asked whether the screening criteria had been discussed with the onsite

licensee staff performing rebaselining reviews of the inservice testing (IST) program and

the FSAR. The engineers inrifcated that such discussions had not taken place. The

I

inspectors subsequently determined that the IST and inservice inspection programs could

have been affected by the seismic review program screening criteria, and that the IST

system engineer had not been aware of the seismic review until after the inspectors

'

questioned the design engineering personnel. While this issue may have eventually been

i

identified by the licensee through supervisory reviews of the results of this seismic review

l

program, the inspectors considered the failure to integrate the seismic review program

'

'

with the IST testing program review a weakness.

The licensee had several ongoing, parallel improvement initiatives which were in

response to previous NRC enforcement actions. These included development of design

'

basis documents, a verification and update of the FSAR, rebaselining the IST program,

reviewing the inservice inspection program, rewriting system operating procedures, and

updating the IST procedures. Changes in system design basis, such as the addition of a

safety-related function to an existing valve, brought about by licensee staff working on

one of these efforts, could negatively affect the other improvement initiatives if not

properly documented and coordinated. The inspectors reviewed the licensee's response

to the latest Systematic Assessment of Licensee Performance, report

No. 50-266/97001; 50-301/97001, and found that the licensee acknowledged the need to

.

control design basis changes when making plant hardware changes, but that there was

l

no specified initiative to control the effects of design basis changes that might occur as

j

the result of analysis or software changes.

The inspectors met with senior licensee management to express the concem that design

engineering staff had been working on a committed corrective action for eleven months

without coordinating their efforts with other interrelated corrective action initiatives. The

inspectors asked whether this was indicative of a broad problem in design engineering, or

was an isolated incident. The licensee managers acknowledged the inspectors' concem,

and were reviewing the issue at the end of the inspection period. The inspectors will

track the licensee's actions to ensure that design basis changes, including those brought

17

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about by analysis, are property documented and communicated as an inspection follow-

up item (IFl 50 266/98006-06(DRP); 50-301/98006-06(DRP)).

c.

Conclusions

Offsite, corporate office-based engineering personnel working on a corrective action

!

commitment initiative to assess the adequacy of a separation of seismically qualified and

l

non-qualified piping systems were performing analyses and taking credit for components

i

to function in a manner that may not have previously been considered in the design basis.

l

The engineers had not evaluated whether such reliance rnight constitute a design basis

change. Additionally, onsite licensee personnel performing concurrent and interrelated

corrective action initiatives had not been informed of the potential design engineering

.

activities that could have affected the results of these other initiatives.

I

E3

Engineering Procedures and Documentation

!

E3.1

Review of Desian Basis and Controls for 125-Volt Direct Current (Vdc) System

i

a.

Inspection Scope (IP 37551)

l

i

l

The inspectors reviewed the design basis document and applicable battery loading

L

calculations for the 125-Vdc system. The review was performed to ensure accuracy of

l

the documents and verify operability of the system relative to the design basis.

l

l

b.

Observations and Findinas

The 125-Vdc battery system is designed to provide service for one hour in the event of a

i

total loss of altemating current voltage at the station (station blackout). During a review

l

of this system, the inspectors asked licensee representatives to provide any additional

!

documentation which may take into account battery loads added to the system since the

latest master calculation was generated.

l

The licensee provided the inspectors with a current listing of the master, individual

l

battery, and additional equipment calculations for the 125-Vdc system. Many of the

additional equipment loads were listed as evaluated but awaiting update to the goveming

battery calculations.

The inspectors held a meeting with the responsible system engineer to discuss the

system loads and calculations. The engineer stated to the inspectors that the process

used to review modification of loads against existing calculations did not prompt the

reviewer to consider other outstanding loads as the result of other modifications affecting

the system, to determine the cumulative effect on the 125-Vdc system. This condition

could have led to concurrent modifications not referencing appropriate updated battery

loading calculations. However, the system engineer subsequently performed

,

l

conservative calculations from the modification documentation available to illustrate that

the 125-Vdc system was operable. The process problems identified were described in

'

CR 98-1528. An OD, written on April 9,1998, indicated that the system was operable.

The inspectors regarded the lack of maintaining accurate documentation of the 125-Vdc

decign basis capabilities a violation (VIO 50-266/98006-07(DRP); 50-301/98006-07(DRP))

of 10 CFR Part 50 Appendix B, Criterion Ill, " Design Control," which requires that design

18

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.

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.

changes be subject to design control measures to assure that the design basis is

maintained. This problem dated back to about May 31,1995, when the calculations for

the Nos.105,106, and 305 station batteries had last been updated. The inspectors

reviewed the OD regarding the issues discussed above and had no further questions on

)

the matter.

1

c.

Conclusions

l

The inspectors concluded that tne 125-Vdc system was capable of meeting design basis

functions. However, the failure to maintain an up-to-date battery loading calculation was

'

considered a violation of 10 CFR Part 50, Appendix B, Criteiion ill, " Design Control."

!

E3.2

Reactor Enaineerina Update of Estimated Cribcal Rate Position Calculation

a.

Inspection Scope (IPs 37551 and 71707)

l

l

The inspectors reviewed the circumstances of the suspended critical approach on

March 28,1998, discussed in Section 01.1 of this report.

I

'

b.

Observations and Findinas

!

As discussed in Section 01.1 of this report, the first attempt to bring the Unit 2 reactor

l

critical on March 28,1998, was suspended due to the licensse's identification during the

3

withdrawal of Control Bank "D" control rods that the reactor would become critical much

earlier than anticipated based on the estimated critical rate calculation. Operations

.

_ personnel followed appropriate procedures regarding this matter. The reactor critical rate

)

l

position was recalculated prior to a second attempt to bring the reactor critical.

i

l

The inspectors reviewed the information regarding the first critical approach to ascertain

l

why the estimated rate calculation was in error. The inspectors leamed through

!

interviews of reactor engineering personnel and a review of a recent reactor engineering

'

self-assessment, that the estimated critical rate position calculation procedure had been

identified as needing revision. In the self-assessment report dated December 3,1997, a

finding highlighted the need for obtaining accurate xenon information from a previous

shutdown to ensure the accuracy of subsequent startup critical parameters. The reactor

engineering organization had not implemented this recommendation prior to the restart of

Unit 2. The inspectors regarded this matter as another example of a problem with reactor

l

engineering performance that resulted in a previous violation

(VIO 50-266/98003-02(DRP); 50-301/98003-02(DRP)).

!

c.

Conclusions

l

The inspectors concluded that the reactor engineering organization provided an

inadequate critical rate position procedure to operations personnel during the startup of

Unit 2. Although reactor engineering personnel had previously identified problems with

the procedure, timely corrective actions had not been taken. The problems revealed

during the startup were considered additional examples of a previously identified problem

with reactor engineering performance, for which a violation had been recently issued.

19

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.

l.

E4

Engineering Staff Knowledge and Performance (IP 37551)

During a vertical slice review of the 125-Vdc system, the inspectors interviewed the

engineer responsible for the system. The discussion involved design bases and

operability considerations for the system. The engineer had been assigned to the system

,

for less than one month.. Nevertheless, the inspectors noted that the engineer displayed

.

clear ownership of the 125-Vdc system and conveyed a sensitivity to emerging issues

affecting the system and aggressively pursued issue resolution.

E6

Engineering Organization and Administration

E6.1

Conduct of the Dutv Technical Advisor Proaram

a.

Inspection Scope (IPs 37551 and 71707)

l

l

As part of the monitoring of the Unit 2 reactor startup on March 28,1998, the inspectors

reviewed the implementation of the duty technical advisor (DTA) program.

b.

Observations and Findinas

On the evening of March 27,1998, during the first attempt to t::ing the Unit 2 reactor

critical, the inspectors noted that the DTA (a reactor engineer) also served as the startup

engineer for the Unit. This individual had been the DTA for the day and was present for

the critical approach which began around 2:00 a.m., on March 28,1998. The DTA had

,

!

been called earlier in the evening to review and verify procedures and calculations for the

)

l

reactor startup. The inspectors queried the DTA as to his alertness and if he had an

opportunity for rest earlier in the evening. The DTA indicated that he was able to get

some brief rest and felt capable to oversee the reactor startup. The inspectors noted no

problems regarding the DTA's performance during the subsequent startup attempt.

The inspectors noted during the second attempt to start up Unit 2 on March 28,1998, at

around 2:00 p.m., that the same individual was serving as the DTA (but not as the startup

engineer). The inspectors asked the DTA about the two consecutive days of work. The

DTA indicated that due to a reduction in the number of qualified DTAs, consecutive days

l

were occasionally required.

Concemed about the appropriateness of DTAs standing 48-hour-long watches, the

inspectors reviewed the licensee's DTA program and response to NRC Generic

l

Letter 86-04, " Policy Statement on Engineering Expertise on Shift." The inspectors noted

that the program was approved by the NRC for DTAs to stand 24-hour watches and that

i

the number of available DTAs would be sufficient for adequate rotation of DTA-qualified

. personnel. The inspectors also noted that the intent of the procedure describing

l

implementation of the DTA program (Nuclear Organization Manual Duty Technical

l

Advisor Procedure) was that DTAs would not serve a collateral position while functioning

l

as a DTA. The inspectors acknowledged to station management that the DTA who

served as the startup engineer for the first critical attempt was not the "on-call" reactor

engineer and that this met the verbatim requirements of the procedure However, the

'

fact that the DTA served as the startup engineer was not in accordance with the intent of

,

the procedure.

20

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,

The inspectors discussed with licensee management the concems regarding DTAs

serving 48-hour shifts and their fitness-for-duty to fulfill their safety-related role in

response to an emergency. Licensee management indicated that oversight of the

'

,

DTA program would be assigned to the operations department manager and that

consecutive shifts would no longer be allowed. The operations manager issued an

'

electronic message to all DTAs regarding this matter, following the discussion with the

inspectors.'

Licensee management also indicated that this issue would be further corrected later in

the year as plans were well underway to establish a shift technical advisor program which

j

would be controlled by the operations department.

c.

. Conclusions

The inspectors concluded that the practice of DTAs serving two consecutive shifts

(48 hours5.555556e-4 days <br />0.0133 hours <br />7.936508e-5 weeks <br />1.8264e-5 months <br />) was not consistent with the intent of program procedures and raised questions

regarding the DTA's fitness-for-duty. Although the inspectors noted no associated

performance issues, licensee management immediately revised expectations to preclude

1

potential fitness-for-duty issues.

E8

Miscellaneous Engineering issues

E8.1

(Closed) VIO 50-266/96002-05(DRP): 50-301/96002-05(DRP): Three examples were

identified regarding the failure to update the FSAR as required by 10 CFR 50.71(e). The

licensee revised the FSAR to address the three examples and subsequently formed an

'j

interdisciplinary process improvement team to review the FSAR update process to ensure

that all required changes were being identified and implemented in a timely manner. One

outcome of the review was a revision of the FSAR change procedure (Nuclear Power

Business Unit Procedure, NP 5.2.6, "FSAR Updates"). However, during a followup

inspection of this area (IR No. 50-266/97023(DRS); 50-301/97023(DRS)), NRC inspectors

identified two additional examples where the FSAR had not been revised in a timely

manner and a violation of 10 CFR Part 50, Appendix B, Criterion XVI, " Corrective Action,"

was cited. The earlier violation is considered closed and the corrective actions for the

failure of the previous long-term corrective actions will be reviewed as part of the more

recent violation (VIO 50-266/97023-03(DRS); 50-301/97023-03(DRS)).

E8.2

(Closed) VIO 50-266/96003-04(DRP): 50-301/96003-04(DRP): Contrary to American

Society of Mechanical Engineers (ASME) Code post-maintenance testing requirements,

service water pump P-32E was retumed to service in December 1995 without

determining a new vibration reference value or confirming the previous reference value.

This issue involved the retum of the pump to service with vibrations in the " alert" range.

In a letter to the NRC dated July 19,1996, the licensee did not agree that this issue was

a violation of ASME Code requirements and did not address what actions were being

taken to prevent reoccurrence of a similar problem. As discussed in a letter to the

licensee from the NRC, dated October 30,1996, the licensee has taken steps to prevent

recurrence.

Early in 1997, inspector review of the repair, testing, and retum-to-service of the P-32A

service water pump identified that the licensee still had a misunderstanding of ASME

Code reference value requirements. This misunderstanding was resolved before the

21

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.

.

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.

pump was retumed to service. Subsequent NRC review of the licensee's inservice

l

testing program in mid-1997 identified no additional problems with reference value

requirements (Section M3.1.b.4, IR No. 50-266/97010(DRS); 50-301/97010(DRS)).

E8.3

(Closed) IFl 50-266/96006-01(DRP): 50-301/96006-01(DRP): The inspectors will review

the results of the licensee's review of the inservice testing program to ensure that design

basis requirements for all safety-related pumps are incorporated in IST program test

i

acceptance criteria. A followup programmatic review of this issue by NRC inspectors

(IR No. 50-266/96013(DRP); 50 301/96013(DRP)) did not identify any problems; howevel,

the inspectors kept the IFl open pending a review of the incorporation of instrument

1

inaccuracies into IST acceptance criteria. In late 1996, the licensee completed

)

I

engineering calculations addressing the incorporation of instrument inaccuracies into the

acceptance criteria. The inspectors reviewed Calculation No. 96-0233 for the

'

containment spray pumps and verified that the instrument inaccuracies had been

1

incorporated into the pump IST acceptance criteria.

Partly because of the concems identified in the past two years by the licensee and the

i

NRC, the licensee initiated an extensive rebaselining of the IST program in mid-1997.

1

The rebaselining effort was being conducted by a team of two full-time contractors, one

part-time contractor, and the site IST program coordinator. A brief description of the

i

rebaselining project was provided to the NRC in a letter dated December 12,1997, from

the licensee. To date, the project has resulted in an extensive rewriting and amplification

of IST background documents and the generation of numerous condition reports.

E8.4

(Closed) LER 50-266/96016: Pressurizer Safety Valve Lift Setpoint Out of Tolerance Due

l

to Temperature Effects. This item was discussed and dispositioned in Sections E8.2

'

and E8.3 of IR No. 50-266/98003(DRP); 50-301/98003(DRP), but the applicable LER was

misidentified as LER 50-266/96014, which had previously been closed. This section

corrects the administrative error (referencing the incorrect LER number) contained in

IR No. 50-266/98003(DRP); 50-301/98003(DRP).

E8.5 LQlosed) LER 50-266/97021: SFP Cooling System Not in Accordance With Plant Design

Basis. This item is discussed and dispositioned in Section E1.2 of this report.

,

l

l

E8.6

(Closed) LER 50-266/97028: RWST Recirculation Piping not in Compliance with Plant

Design Basis. This item is discussed and dispositioned in Section E1.2 of this report.

l

IV. Plant Support

R1

Radiological Protection and Chemistry (RP&C) Controls

R1.1

Unit 1 Refuelino Outaae Radiological Controls Performance Durina This inspection Period

'

(IP 71750)

The licensee had recorded 85 person-rem for the Unit 1 refueling outage at the end of the

inspection period. This was on track with established goals which projected the outage

personnel exposures to total about 130 person-rem. Personnel contamination events

(PCEs) were much higher than anticipated with 81 recorded at the end of the inspection

period. The goal for the entire outage was set at 63 PCEs. Most of the PCEs were low-

l

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.

.

level contaminations (shoes); however, the health physics department was in the process

of evaluating the potential causes for the higher than expected number of PCEs. The

inspectors concluded that the licensee was maintaining good radiological controls for the

Unit i refueling outage and an appropriate response was being undertaken to address

higher than anticipated PCEs.

R7

Quality Assurance in RP&C Activities

R7.1

Quality Assurance Audit of Health Physics Exit Meetina (IP 7175,0.]

The inspectors attended a quality assurance department audit exit meeting on April 6,

1998. The audit included a review of various aspects of the radiation protection program

including, instrumentation controls, offsite dose calculation manual adequacies, radiation

protection personnel training, and implementation of personnel dosimeter programs. The

auditors identified several findings within these areas which were both administrative and

performance-based. The radiation protection program manager openly discussed the

findings with the auditors to gain a clear understanding of the issues. The results of this

audit will be contained in audit report A-P-98-03 which was not issued at the end of the

inspection period.

V. Manaaement Meetinas

X1

Exit Meeting Summary

The inspectors presented the inspection results to members of licensee management at the

conclusion of the inspection on April 17,1998. The licensee acknowledged the findings

presented. The inspectors asked the licensee whether any materials examined during the

inspection should be considered proprietary. No proprietary information was identified.

X3

Meeting With Local Public Officials

The inspectors, along with the Senior Resident inspector from the Kewaunee Nuclear Power

Plant, met with local officials from the Town of Two Creeks, Kewaunee County, and Manitowoc

County on Thursday April 16,1998, at the Two Creeks Town Hall in Two Creeks, Wisconsin.

The inspectors provided the officials with an overview of NRC organizations, the resident

inspector program, and the inspection process. Local officials asked the inspectors questions

i

regarding these matters and other aspects of the NRC, which were answered by the inspectors.

i

The officials thanked the inspectors for the opportunity to meet and ask questions.

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.

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PARTIAL LIST OF PERSONS CONTACTED

Licensee

Wisconsin Electric Power Company M/EPCO)

S. A. Patuiski, Site Vice President

A. J. Cavia, Plant Manager (outgoing)

M. E. Reddemann, Plant Manager (incoming)

R. G. Mende, Operations Manager

W. B. Fromm, Maintenance Manager

J. G. Schweitzer, Site Engineering Manager

R. P. Farrell, Health Physics Manager

D. F. Johnson, Regulatory Services and Licensing Manager

24

_ _ _ _ - _ - _ _ - _ _ _ _ _ - _ _ _ _ _ _ _ _ _

t

.

INSPECTION PROCEDURES USED

IP 37551:

Onsite Engineering

IP 40500:

Effectiveness of Licensee Controls in identifying, Resolving, and Preventing

Problems

IP 61726:

Surveillance Observations

IP 62707:

Maintenance Observations

IP 71707:

Plant Operations

IP 71750:

Plant Support Activities

IP 92700:

Onsite Follow up of Written Reports of Noaroutine Events at Power Reactor

Facilities

ITEMS OPENED, CLOSED, AND DISCUSSED

Opened

50-266/98006-01(DRP)

VIO

Failure to follow the procedure regarding reactor

operator observations of the main control panels

50-266/98006-02(DRP)

VIO

Failure to follow the procedure regarding the

weighing of the reactor vessel intemals lifting rig

50-301/98006-03(DRP)

NCV

Failure to perform post maintenance testing prior to

placing LTOP in service

50-301/98006-04(DRP)

NCV

Failure tu implement corrective action regarding C-

036

50-266/98006-05(DRP)

NCV

Design control of seismically controlled piping

50-301/98006-05(DRP)

systems related to SFP and RWST

50-266/98006-06(DRP)

IFl

Followup of design basis changes to ensure

50-301/98006-06(DRP)

proper documentation and interdepartmental

I

communications

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50-266/98006-07(DRP)

VIO

Failure to implement adequate design control

50-301/98006-07(DRP)

measures for 125-Vdc system calculations

i

Closed

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50-266/98004

LER

Reactor coolant pump lube oil collection system

50-301/98004

design nonconformance with Appendix R

Section 111.0

50-301/98002

LER

Reactor coolant pump component cooling water

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retum line check valve seriously degraded

25

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50-301/95006

LER

PORV post-maintenance testing not performed prior

to establishing LTOP

50-301/98006-02(DRP)

NCV

Failure to perform post maintenance testing prior to

i

placing LTOP in service

50-266/96002-01(DRP)

IFl

Scheduling and planning of work

50-301/96002-01(DRP)

50-266/97042

LER

Failure to perform containment personnel air lock

surveillance

(

50-301/98006-03(DRP)

NCV

Failure to implement corrective action regarding C-

'

036

50-266/98006-04(DRP)

NCV

Design control of seismically controlled piping

50-301/98006-04(DRP)

systems related to SFP and RWST

l

50-266/96002-05(DRP)

VIO

Licensees program weakness to update FSAR

'

50-301/96002-05(DRP)

50-266/%003-04(DRP)

VIO

IST Weakness - ASME Code

50-301/96003-04(DRP)

50-266/96006-01(DRP)

IFl

IST Program deficiencies

l

50-301/96006-01(DRP)

50-266/% 016

LER

Pressurizer safety valve lift set point out of tolerance

due to temperature effects

50-266/97021

LER

Spent fuel pool cooling system not in accordance

j

with plant design basis

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50-266/97028

LER

Refueling water storage tank recirculation piping not

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in compliance plant design basis

Discussed

50-266/97020-02(DRP)

IFl

Evaluate procedure upgrade program

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50-301/97020-02(DRP)

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50-266/97006-02(DRP)

IFl

Review maintenance program improvements

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50-301/97066-02(DRP)

50-266/97021-02(DRP)

VIO

Failure to test containment door interlock

50-301/97021-02(DRP)

l

50-266/97023-03(DRS)

VIO

Failure of corrective actions for FSAR updates

50-301/97023-03(DRS)

26

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. _ _ _

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.

.

.

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LIST OF ACRONYMS USED IN POINT BEACH REPORTS

AC

Altemating Current

AFW

Auxiliary Feedwater

ASME

American Society of Mechanical Engineers

I

CCW

Component Cooling Water

CFR

Code of Federal Regulations

CLB

Current Licensing Basis

CO

Control Operator

CR

Condition Report

DOS

Duty Operating Supervisor

j

DRP

Division of Reactor Projects

DTA

Duty Technical Advisors

ECCS

Emergency Core Cooling System

,

EDG

Emergency Diesel Generator

l

ESF

Engineered Safety Feature

'

EP

Emergency Planning

FSAR-

Final Safety Analysis Report

IFl

inspection Follow-up Item

IP

Inspection Procedure

IPE

Individual Plant Evaluation

l

IR

inspection Report

lLRT

Integrated Leak Rate Test

IST

Inservice Testing

IT

'7 service Test Procedure

LCO

Limiting Condition for Operation

LER

Licensee Event Report

LTOP

Low Temperature Over-Pressure Protection

NCV

Non-Cited Violation

NDE

Non-Destructive Examination

l

NP

Nuclear Power Business Unit Procedures

j

'

NRC

Nuclear Regulatory Commission

OD

Operability Determination

01

Operating Instruction

OM

Operations Manual

j

OOS

Out-of-Service

i

'

OP

Operating Procedure

ORT

Operations Refueling Test

PASS

Post-accident Sampling System

PCE

Personnel Contamination Event

POD

Prompt Operability Determination

'

PORV

Power-Operated Relief Valve

QA

Quality Assurance

RCP

Reactor Coolant Pump

RCS

Reactor Coolant System

RHR

Residual Heat Removal

RMP

Routine Maintenance Procedure

RP

Radiation Protection

RV

Reactor Vessel

RWST

Refueling Water Storage Tank

27

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___. -. --

-.

.

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SE

Safety Evaluation

SER

Safety Evaluation Report

SFP

Spent Fuel Pool

'

SW

Service Water

TDAFW

Turbine Driven Auxiliary Feedwater

TS

Technical Specification

)

T/S

Technical Specification Test

URI

Unresolved item

Vdc

Volt Direct Current

VIO

Violation

VNCR

Control Room Ventilation

1

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28

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S. Patuiski

-2-

i

The violations identified above are cited in the enclosed Notice of Violation (Notice), and the

j

circumstances surrounding the violations are described in detailin M e enclosed report. Please

note that you are required to respond to this letter and 5:iould follow the instructions specified in

the enclosed Notice when preparing your response. Tns NRC will use your response, in part, to

determine whether further enforcement action is necesnary to ensure compliance with regulatory

requirements.

In accordance with 10 CFR 2.790 of the NRC's " Rules of Practic'.," a copy of this letter, its

enclosures, and your response will be placed in '.he NRC Public Document Room.

Sir cerely,

/s/ Marc L. Dapas for

Geoffrey E. Grant, Director

Division of Reactor Projects

Docket Nos.: 50-266, 50-301

License Nos.: DPR-24, DPR-27

l

Enclosures:

1.

Notice of Violation

2.

Inspection Report

No. 50-266/98006(DRP);

50-301/98006(DRP)

See Attached Distribution

DOCUMENT NAME: G:\\poin\\ poi 98006.drp

To receive a copy of thle document, Indicate in the b3x "C" = Copy without attachment / enclosure "E" = Copy with attachment / enclosure

  • N* = No copy

OFFICE

Rlli

(;-

Rlli

(,

Rlll

,

NAME

Kunowski:dp /fAL JMcBp)pfg

Grant ///

k

DATE

GM98

N/d98

04H95 05/05//P

'

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OFFICIAL RECORD COPY

1

L

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_ _ _ _ _ _ _ _ _ _ _ _ _ _ _ - _ _ _ _ _ _ _ _ _ _ _ _ - - _ - _ _ _ _ - . - - _ _ _ . - - - _ _ _ _ _ _ - _ _ ,

.

!

.

,

S. Patuiski

-3-

cc w/encis:

R. R. Grigg, President and Chief

Operating Officer, WEPCO

l

A. J. Cayia,' Plant Manager

B. D. Burks, P.E., Director

l

- Bureau of Field Operations

'

Cheryl L. Parrino, Chairman

Wisconsin Public Service

Commission

State Liaison Officer

Distribution:

CAC (E-Mail)

Project Mgr., NRR w/ encl

A. Beati w/ encl

J. Caldwell w/ encl

B. Clayton w/ encl

SRI Point Beach w/enci

)

DRP w/enci

)

TSS w/enct

DRS (2) w/encI

.

Rill PRR w/enci

I

l'

PUBLIC IE-01 wienc!

Docket File w/enci

-

GREENS

LEO (E-Mail)

DOCDESK (E-Mail)

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