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{{#Wiki_filter:--     -                       -                         -         _   -   _.
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          pn Rico                                       UNITED STATES
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      f             'o                       NUCLEAR REGULATORY COMMISSION
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                  / ,^S                                     REGION 11
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    Eet'I *$  k  I
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                                                  101 MARIETTA STREET. N.W.
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              -
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                      f                             ATLANTA, GEORGI A 30323
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      % .' ,',#,. *                                    SEP 2 31985
UNITED STATES
      Report Nos. 50-325/85-27 and 50-324/85-27
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      Licensee: Carolina Power and Light Company
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                        P. O. Box 1551
NUCLEAR REGULATORY COMMISSION
                        Raleigh, NC 27602
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REGION 11
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101 MARIETTA STREET. N.W.
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ATLANTA, GEORGI A 30323
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SEP 2 31985
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Report Nos. 50-325/85-27 and 50-324/85-27
Licensee: Carolina Power and Light Company
P. O. Box 1551
Raleigh, NC 27602
1
1
      Docket Nos.:         50-325 and 50-324                           License Nos.           DPR-71 and DPR-62
Docket Nos.:
      Facility Name: Brunswick 1 and 2
50-325 and 50-324
      Inspection Co                 ed:   ugust 1 ; 31,1985
License Nos.
      Inspectors:           -
DPR-71 and DPR-62
                                      \                                                                      W [
Facility Name: Brunswick 1 and 2
                h L.               arner                     _                                    Vate figned
Inspection Co
                              *
ed:
                                                            "
ugust 1 ; 31,1985
                                                                                                      j M         $4
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      Approved By:                -    /                                                             7       [fd'
Inspectors:
                        P. E. Fredrickson, Section Chief                                           Dite Signed
-
                        Division of Reactor Projects
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                                                          SUMMARY
arner
      Scope: This routine safety inspection involved 177 inspector-hours on site in
Vate figned
      the areas of maintenance observation, surveillance observation, operational
_
      safety verification, onsite review committee, ESF System walkdown, Licensee Event
j M
      Reports review, follewup on inspector identified items, refueling activities and
$4
      plant modifications.
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      Results:       One violation was identified: Bolts Replaced on Hydraulic Control
h T. E.
      Units with Type Other Than That Specified on Drawings. One unresolved item was
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      identified:         Seismic Qualification of Hydraulic Control Unit Frame.
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Approved By:
-
P. E. Fredrickson, Section Chief
Dite Signed
Division of Reactor Projects
SUMMARY
Scope: This routine safety inspection involved 177 inspector-hours on site in
the areas of maintenance observation, surveillance observation, operational
safety verification, onsite review committee, ESF System walkdown, Licensee Event
Reports review, follewup on inspector identified items, refueling activities and
plant modifications.
Results:
One violation was identified:
Bolts Replaced on Hydraulic Control
Units with Type Other Than That Specified on Drawings. One unresolved item was
identified:
Seismic Qualification of Hydraulic Control Unit Frame.
I
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      h0040510850923
h0040510850923
    G         ADOCK 05000324
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                                    PDR
ADOCK 05000324
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                      ._     ..._ ___. .                 ._.                 - . - - - .     ._ __ _                                   - _. _ __
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                                                              REPORT DETAILS
._ __ _
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REPORT DETAILS
!
!
                    1.   Licensee Employees
1.
Licensee Employees
Persons Contacted
,
,
                          Persons Contacted
P. Howe, Vice President - Brunswick Nuclear Project
.
.
                          P. Howe, Vice President - Brunswick Nuclear Project
C. Dietz, General Manager - Brunswick Nuclear Project
                          C. Dietz, General Manager - Brunswick Nuclear Project
T. Wyllie, Manager - Engineering and Construction
,                        T. Wyllie, Manager - Engineering and Construction
,
                          G. Oliver, Manager - Site Planning and Control
G. Oliver, Manager - Site Planning and Control
!                         J. Holder, Manager - Outages
!
l                         E. Bishop, Assistant to General Manager                                                                                   I
J. Holder, Manager - Outages
i                         L. Jones, Director - QA/QC                                                                                                 r
l
                          M. Shealy, Acting Director - Training                                                                                     ,
E. Bishop, Assistant to General Manager
;                        M. Jones, Acting Director - Onsite Nuclear Safety - BSEP
I
'
i
                          J. Chase, Manager - Operations
L. Jones, Director - QA/QC
                          J. O'Sullivan, Manager - Maintenance
r
M. Shealy, Acting Director - Training
,
,
                          G. Cheatham, Manager - Environmental & Radiation Control
;
4                        K. Enzor, Director - Regulatory Compliance
M. Jones, Acting Director - Onsite Nuclear Safety - BSEP
                          B. Hinkley, Manager - Technical Support
J. Chase, Manager - Operations
                          L. Boyer, Director - Administrative Support
'
;                        V. Wagoner, Director - IPBS/Long Range Planning
J. O'Sullivan, Manager - Maintenance
L                        C. Blackmon, Superintendent - Operations
G. Cheatham, Manager - Environmental & Radiation Control
j                        J. Wilcox, Principle Engineer - Operations
                          W. Hogle, Engineering Supervisor
,
,
                          W. Tucker, Engineering Supervisor
;                        B. Wilson, Engineering Supervisor
                          R. Creech, I&C/ Electrical Maintenance Supervisor (Unit 2)
                          J. Moyer, I&C/ Electrical Maintenance Supervisor (Unit 1)
                          R. Kitchen, Mechanical Maintenance Supervisor (Unit 2)
                          R. Poulk, Senior.NRC Regulatory Specialist
                          D. Novotny, Senior Regulatory Specialist
4
4
                          W. Dorman, QA - Supervisor
K. Enzor, Director - Regulatory Compliance
                          W. Hatcher, Security Supervisor
B. Hinkley, Manager - Technical Support
.                       W. Murray, Senior Engineer - Nuclear Licensing Unit
L. Boyer, Director - Administrative Support
                          Other licensee employees contacted included construction craftsmen,
;
                          engineers, technicians, operators, office personnel, and security force
V. Wagoner, Director - IPBS/Long Range Planning
L
C. Blackmon, Superintendent - Operations
j
J. Wilcox, Principle Engineer - Operations
W. Hogle, Engineering Supervisor
W. Tucker, Engineering Supervisor
,
;
B. Wilson, Engineering Supervisor
R. Creech, I&C/ Electrical Maintenance Supervisor (Unit 2)
J. Moyer, I&C/ Electrical Maintenance Supervisor (Unit 1)
R. Kitchen, Mechanical Maintenance Supervisor (Unit 2)
R. Poulk, Senior.NRC Regulatory Specialist
D. Novotny, Senior Regulatory Specialist
W. Dorman, QA - Supervisor
4
W. Hatcher, Security Supervisor
.
W. Murray, Senior Engineer - Nuclear Licensing Unit
Other licensee employees contacted included construction craftsmen,
engineers, technicians, operators, office personnel, and security force
members.
,
,
                          members.
!
!
;                   2.   Exit Interview (30703)                                                                                                     i
;
                          The inspection scope and findings were summarized on September 5, 1985 with
2.
;                        the general manager. The licensee acknowledged the findings without
Exit Interview (30703)
i                         exception.       The licensee did not identify as proprietary any of the
i
j                         materials provided to or reviewed by the inspectors during the inspection.
The inspection scope and findings were summarized on September 5, 1985 with
                    3.   Followup on' Previous Enforcement Matters (92702)
the general manager.
                          Not inspected.
The licensee acknowledged the findings without
;
i
exception.
The licensee did not identify as proprietary any of the
j
materials provided to or reviewed by the inspectors during the inspection.
3.
Followup on' Previous Enforcement Matters (92702)
Not inspected.
.
. - _ . . . - ,
- ..
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.
    . - _ . . . - ,              - ..    .
- - . - - -
                                              - - . - - -       . . _ - . , ,       . . - . -         - _ - , , . - - - - . ,- ,,.-.-,.
. . _ - . , ,
. . - . -
- _ - , , . - - - - . ,- ,,.-.-,.


      _                   ..
_
        .
..
    a
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                                                                    2
a
2
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        4. Followup on Inspector Followup Items
4.
          a.   (Closed) Inspector Followup Item 325, 324/84-35-02; Post Trip Reviews
Followup on Inspector Followup Items
                01-22. An open item was generated after a reactor scram in December
a.
                1984 because of a questionable post trip review. The item was to
(Closed) Inspector Followup Item 325, 324/84-35-02; Post Trip Reviews
                follow the licensee's progress toward enhancing the scram review
01-22. An open item was generated after a reactor scram in December
                process.     Revisions 8-10 to the Post Trip Review Procedure 01-22 were
1984 because of a questionable post trip review.
                the result of this effort.                       These revisions clarify the responsibili-
The item was to
                ties of the operations engineer and other associated requirements.
follow the licensee's progress toward enhancing the scram review
                This item is considered closed.
process.
          b.   (Closed)       Inspector   Followup                   Item 324/84-31-03; Standby Air
Revisions 8-10 to the Post Trip Review Procedure 01-22 were
                Compressors.     This item was opened because of a concern over the
the result of this effort.
                inoperability of an automatic start pressure switch for a standby air
These revisions clarify the responsibili-
                compressor.     The licensee has failed to find a suitable replacement,
ties of the operations engineer and other associated requirements.
This item is considered closed.
b.
(Closed)
Inspector
Followup
Item
324/84-31-03;
Standby Air
Compressors.
This item was opened because of a concern over the
inoperability of an automatic start pressure switch for a standby air
compressor.
The licensee has failed to find a suitable replacement,
I
I
                but is presently undertaking a plant modification on Unit 1 (and is
but is presently undertaking a plant modification on Unit 1 (and is
                planned on Unit 2) which will alleviate the need for these air
planned on Unit 2) which will alleviate the need for these air
::               compressors during post accident conditions.                       The modification will
::
                install a nitrogen backup system which will supply the necessary
compressors during post accident conditions.
The modification will
install a nitrogen backup system which will supply the necessary
.
.
                pneumatic pressure during accident conditions. This item is considered
pneumatic pressure during accident conditions. This item is considered
!               closed.
!
  I
closed.
          c.   (Closed) Inspector Followup Item 325, 324/85-03-01; Radwas*e Shipping.
I
                This item was generated to track improvements in the radwaste shipping                     ,
c.
                quality control program and the auditing of this program. This item is
(Closed) Inspector Followup Item 325, 324/85-03-01; Radwas*e Shipping.
                considered closed because a notice of violation 325, 324/85-17-01 was
This item was generated to track improvements in the radwaste shipping
                written in this area and will track corrective actions.
,
        5. Maintenance Observation (62703)
quality control program and the auditing of this program. This item is
          The inspectors observed maintenance activities and reviewed records to
considered closed because a notice of violation 325, 324/85-17-01 was
          verify that work was conducted in accordance with approved procedures,
written in this area and will track corrective actions.
:         Technical Specifications, and applicable industry codes and standards. The
5.
          inspectors also verified that:                           redundant components were operable;
Maintenance Observation (62703)
j         administrative controls were followed; tagouts were adequate; personnel were
The inspectors observed maintenance activities and reviewed records to
,
verify that work was conducted in accordance with approved procedures,
          qualified; correct replacement parts were used; radiological controls were
:
          proper; fire protection was adequate; QC hold points were adequate and
Technical Specifications, and applicable industry codes and standards. The
          observed; adequate post-maintenance testing was performed; and independent
inspectors also verified that:
          verification requirements were implemented. The inspectors independently
redundant components were operable;
4
j
          verified that selected equipment was properly returned to service.
administrative controls were followed; tagouts were adequate; personnel were
          Outstanding work requests and authorizations (WR&A) were reviewed to ensure
qualified; correct replacement parts were used; radiological controls were
          that the licensee gave priority to safety-related maintenance.
,
          a.   Bolting Replacement and Seismic Qualification of Hydraulic Contr^1
proper; fire protection was adequate; QC hold points were adequate and
                Units
observed; adequate post-maintenance testing was performed; and independent
verification requirements were implemented.
The inspectors independently
verified that selected equipment was properly returned to service.
4
Outstanding work requests and authorizations (WR&A) were reviewed to ensure
that the licensee gave priority to safety-related maintenance.
a.
Bolting Replacement and Seismic Qualification of Hydraulic Contr^1
Units
Inspection Report 325/85-22- issued a notice of violation for loose
<
<
                Inspection Report 325/85-22- issued a notice of violation for loose
and/or missing rack-support-to-foundation bolting for the control rod
                and/or missing rack-support-to-foundation bolting for the control rod
!
!               hydraulic control units (HCU). During followup of the repair and
hydraulic control units (HCU).
                replacement, it was observed by the inspector that all the replaced
During followup of the repair and
replacement, it was observed by the inspector that all the replaced
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                        _   ,         _     _ _ - , _ _ , _ _ _
_
,
_
_ _ - , _ _ , _ _ _
_____
,_. _


    .
.
  .
.
                                                  3
3
                                                                                                                  !
!
                                                                                                                  !
!
        bolts (five) had been replaced with bolts which were not cadmium plated
bolts (five) had been replaced with bolts which were not cadmium plated
        as required by plant design drawing G.E. 919D615. The apparent root
as required by plant design drawing G.E. 919D615.
,        cause was that the maintenance planner verified that Q bolting was
The apparent root
        required but failed to check the specifications for any special
cause was that the maintenance planner verified that Q bolting was
        requirements. Discussion with licensee personnel indicates that this
,
        may have been a common practice when replacing bolting. The licensee
required but failed to check the specifications for any special
        is currently evaluating the impact of this on plant equipment.
requirements.
        Failure to install the type of bolting specified on G.E. 9190615
Discussion with licensee personnel indicates that this
        drawing is a violation of 10 CFR 50, Appendix B,                           Criterion V
may have been a common practice when replacing bolting. The licensee
        (324/85-27-01): Bolts Replaced on Hydraulic Control Units with Type
is currently evaluating the impact of this on plant equipment.
        Other than that Specified on Drawings.
Failure to install the type of bolting specified on G.E. 9190615
        The licensee has attempted to establish the seismic qualification of
drawing is a violation of 10 CFR 50, Appendix
        the as-found conditions documented in inspection report 325/85-22,
B,
        i.e., one HCU had 2 out of the 4 rack-support-to-foundation bolts
Criterion V
        missing. Calculations were performed on the HCU's with missing bolts,
(324/85-27-01):
        on HCU's which stand alone and on HCU's installed back-to-back with all
Bolts Replaced on Hydraulic Control Units with Type
        fasteners properly installed. The calculations show the as found HCU's
Other than that Specified on Drawings.
        with loose or missing bolts met at least short term criteria (IEB
The licensee has attempted to establish the seismic qualification of
        79-14),   i.e.,       bolts might deform but would not break.                 The same
the as-found conditions documented in inspection report 325/85-22,
        conclusion was deterrrined for the stand alone HCU's. However, in all
i.e., one HCU had 2 out of the 4 rack-support-to-foundation bolts
        cases including back-to-back installation, stresses were calculated
missing. Calculations were performed on the HCU's with missing bolts,
        which exceeded the allowable stress in the tubular frame. The original
on HCU's which stand alone and on HCU's installed back-to-back with all
fasteners properly installed. The calculations show the as found HCU's
with loose or missing bolts met at least short term criteria (IEB
79-14),
i.e.,
bolts might deform but would not break.
The same
conclusion was deterrrined for the stand alone HCU's. However, in all
cases including back-to-back installation, stresses were calculated
which exceeded the allowable stress in the tubular frame. The original
i
i
        seismic qualification was performed by the vendor (G.E.) based upon
seismic qualification was performed by the vendor (G.E.) based upon
        results of field tests with the units tested back-to-back. This field
results of field tests with the units tested back-to-back. This field
        test data is not available to the licensee at this time. Without field
test data is not available to the licensee at this time. Without field
        test data, the complexity of the installed configuration requires
test data, the complexity of the installed configuration requires
        several conservative assumptions to be made to allow analytic modeling.
several conservative assumptions to be made to allow analytic modeling.
        The licensee believes that their calculated results are conservative.
The licensee believes that their calculated results are conservative.
        Therefore, since the frame was qualified by the vendor from experi-
Therefore, since the frame was qualified by the vendor from experi-
        mental data, the licensee believes the frames to be qualified and the
mental data, the licensee believes the frames to be qualified and the
        HCU's are operable, i.e. seismically qualified. However, the licensee
HCU's are operable, i.e. seismically qualified. However, the licensee
        expects to resolve this apparent discrepancy between their analytic
expects to resolve this apparent discrepancy between their analytic
        model and the original seismic qualification based on field data.
model and the original seismic qualification based on field data.
Resolution of this apparent discrepancy is an unresolved item
1
1
        Resolution of this apparent discrepancy is an unresolved item
(325/85-27-01 and 324/85-27-02):
        (325/85-27-01 and 324/85-27-02):           Seismic Qualification of HCU Frame,
Seismic Qualification of HCU Frame,
      b. Post Maintenance Test Requirement Test Sheet Fails to Specify Pressure
b.
        Test /VT-2 Inspection
Post Maintenance Test Requirement Test Sheet Fails to Specify Pressure
Test /VT-2 Inspection
During a routine inspection of post maintenance surveillance testing
,
,
'
'
        During a routine inspection of post maintenance surveillance testing
for the Unit I standby liquid control injection check valve C41-F007,
        for the Unit I standby liquid control injection check valve C41-F007,
the inspector noticed that no pressure test /VT-2 inspection was
        the inspector noticed that no pressure test /VT-2 inspection was
specified on the Post Maintenance Test Requirement (PMTR) sheet even
        specified on the Post Maintenance Test Requirement (PMTR) sheet even
though the pressure boundary for the valve had been broken during
        though the pressure boundary for the valve had been broken during
maintenance. The valve is Class 1.
Two similar maiatenance activities
4
4
        maintenance. The valve is Class 1. Two similar maiatenance activities
involving Class 1 valves B21-F028B and B21-F019 were also reviewed and
        involving Class 1 valves B21-F028B and B21-F019 were also reviewed and
found to not contain the pressure test /VT-2 inspection requirement on
        found to not contain the pressure test /VT-2 inspection requirement on
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                              '
'
4
4
                      - - - . ,             -. -             -         ,-, - _ - - -         -- -- ,- - - - - -
- - - . ,
-. -
-
,-, - _ - - -
-- -- ,- - - - - -


                    _ -       _ _ _               .-     -- . _ = - -                         -             . _ _ - - _ _ .
_ -
                                                                                                                                    - - - .   _. .
_ _ _
        *
.-
-- . _ = - -
-
. _ _ - - _ _
- - - .
_.
.
.
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    .
.
                                                                        4
4
                        the PMTR sheet. It became clear that the maintenance planners were not
the PMTR sheet. It became clear that the maintenance planners were not
                        using ENP-16, Inservice Inspection Requirements, properly. After
using ENP-16, Inservice Inspection Requirements, properly.
                        scoping the jobs and realizing that the work involved disassembly of
After
                        the valves, the planners should have realized that the pressure
scoping the jobs and realizing that the work involved disassembly of
                        boundaries of each of these valves was to be broken and that entry into
the valves, the planners should have realized that the pressure
                        Section VI, Visual Inspection, of ENP-16 was necessary to determine
boundaries of each of these valves was to be broken and that entry into
                        additional post maintenance test requirements. This process was not
Section VI, Visual Inspection, of ENP-16 was necessary to determine
,
additional post maintenance test requirements.
                        done.
This process was not
i                       The problem was discussed with plant management and the following
done.
!
,
                        immediate corrective actions were taken:
i
'
The problem was discussed with plant management and the following
                        (1) Training was conducted for all mechanical maintenance planners in
!
                                the proper use of ENP-16.
immediate corrective actions were taken:
                        (2) A review was conducted of PMTR's for Class 1 valves worked during
(1) Training was conducted for all mechanical maintenance planners in
                                the Unit 1 outage. For those which required pressure test /VT-2
'
                                inspections, an additional test / inspection was included on the
the proper use of ENP-16.
                                PMTR sheet. Those activities already closed out, were reopened by
(2) A review was conducted of PMTR's for Class 1 valves worked during
                                an additional PMTR sheet stating the required test.
the Unit 1 outage.
                              At the completion of the present Unit 1 outage, a vessel
For those which required pressure test /VT-2
                                hydrostatic test and inspection including all Class 1 piping and
inspections, an additional test / inspection was included on the
                              components is to be performed (PT-80.1, 10 year Inservice
PMTR sheet. Those activities already closed out, were reopened by
                                Inspection Reactor Vessel Hydrostatic Test). This test would have
an additional PMTR sheet stating the required test.
                                satisfied the inservice inspection requirements for the valves
At the completion of the present Unit 1 outage, a vessel
hydrostatic test and inspection including all Class 1 piping and
components is to be performed (PT-80.1, 10 year Inservice
Inspection Reactor Vessel Hydrostatic Test). This test would have
satisfied the inservice inspection requirements for the valves
;
;
-
identified. Followup of long term corrective actions will be an
                                identified. Followup of long term corrective actions will be an
-
                                inspector followup item (IFI 325/85-27-02): Administrative
inspector followup
!.                             Control Changes to Ensure Pressure Test /VT-2 Inspections are
item (IFI 325/85-27-02): Administrative
                                Identified as Post Maintenance Requirements.
!.
f       6.         Surveillance Observation (61726)
Control Changes to Ensure Pressure Test /VT-2 Inspections are
l
Identified as Post Maintenance Requirements.
)                 The inspectors observed surveillance testing required by Technical
f
:                 Specifications. Through observation and record review, the inspectors
6.
                  verified that:                     tests conformed to Technical Specification requirements;
Surveillance Observation (61726)
                  administrative controls were followed; personnel were qualified;
l
                  instrumentation was calibrated; and data was accurate and complete. The
)
The inspectors observed surveillance testing required by Technical
:
Specifications.
Through observation and record review, the inspectors
verified that:
tests conformed to Technical Specification requirements;
administrative
controls were
followed;
personnel
were
qualified;
instrumentation was calibrated; and data was accurate and complete.
The
inspectors independently verified selected test results and proper return to
4
4
                  inspectors independently verified selected test results and proper return to
service of equipment.
                  service of equipment.
A special review was performed of the following Licensee finding:
                A special review was performed of the following Licensee finding:
On August 21, 1985, the Maintenance Surveillance Test (MST) rewrite group
                  On August 21, 1985, the Maintenance Surveillance Test (MST) rewrite group
discovered that Periodic Tests, PT-A22.2-1,
                  discovered that Periodic Tests, PT-A22.2-1,                                     PT-22.2-2, PT-A24.2 and
PT-22.2-2,
                  PT-45.2.4, covering Secondary Containment Isolation Response Time Testing,
PT-A24.2 and
                  did not adequately test all the relays in the associated logic circuit.
PT-45.2.4, covering Secondary Containment Isolation Response Time Testing,
did not adequately test all the relays in the associated logic circuit.
,
,
Technical Specification Surveillance 4.3.2.3 requires that this be done
'
'
                  Technical Specification Surveillance 4.3.2.3 requires that this be done
every 18 months.
                  every 18 months.
:
:
i
i
      , - , , - .         ,_       -, _ _ . _ . _                   _   _ _ _ _
,
                                                                                  _ ~ - . _ . _ _      ..-..__.                 ._,
-
                                                                                                                                  -
, , - .
                                                                                                                                            ,      .
,_
-, _ _ . _ . _
_
_ _ _ _
~ - .
.
..-..__.
._,
,
.
-


    _           . - - _                     .                         ,       .     _     _                                 _       .     _- -
_
. - - _
.
,
.
_
_
_
.
_- -
4
4
                          .
.
              i
i
    - J
- J
          ,
5
                                                                                  5                                                                            !
,
                            Specifically, relays K66, K67, 3AA, 3AB, 3BA, 3BB, 3BD, A-CRMX and B-CRMX
Specifically, relays K66, K67, 3AA, 3AB, 3BA, 3BB, 3BD, A-CRMX and B-CRMX
  ,/                         were not being included in the response time test. At the time, Unit I was
,/
                            shutdown for a refueling outage (no core alterations were in progress) and
were not being included in the response time test. At the time, Unit I was
shutdown for a refueling outage (no core alterations were in progress) and
Unit 2 was at 100% power.
The surveillance test problem involved both
>
>
                            Unit 2 was at 100% power. The surveillance test problem involved both
units.
                            units.
4
4
                            Licensee management conducted a Plant Nuclear Safety Committee (PNSC)
Licensee management conducted a Plant Nuclear Safety Committee (PNSC)
                            meeting concerning this problem and concluded that there was no technical
meeting concerning this problem and concluded that there was no technical
                            reason to consider this instrumentation inoperable based on the following:
reason to consider this instrumentation inoperable based on the following:
  ,
,
                            a.       Relays not presently being timed have been verified operable in logic
a.
Relays not presently being timed have been verified operable in logic
4
4
                                      system functional tests which were performed in October 1984 (Unit 2).
system functional tests which were performed in October 1984 (Unit 2).
                            b.       The manufacturer's expected response time for these relays is less than
b.
                                      85 milliseconds.
The manufacturer's expected response time for these relays is less than
                            c.       The allowed response time for the instrumentation is less than or equal
85 milliseconds.
                                      to 13 seconds. Adding the relay's expected response time to the
c.
                                      existing instrumentation response time still results in a response time
The allowed response time for the instrumentation is less than or equal
                                      of less than or equal to 1 second.
to 13 seconds.
                            A special test procedure was generated to test the relays (SP-85-086) and
Adding the relay's expected response time to the
                            'was satisfactorily performed for Units i and 2 on August 25, 1985.
existing instrumentation response time still results in a response time
                                                                                                                                                              ,
of less than or equal to 1 second.
                            These inadequate procedures constitute a violation of Technical Specifi-
A special test procedure was generated to test the relays (SP-85-086) and
i.                           cation Surveillance 4.3.2.3,.in that they failed to adequately response time
'was satisfactorily performed for Units i and 2 on August 25, 1985.
1,                           test all the necessary relays. However,10 CFR i Appendix C, Section V,
,
These inadequate procedures constitute a violation of Technical Specifi-
i.
cation Surveillance 4.3.2.3,.in that they failed to adequately response time
1,
test all the necessary relays. However,10 CFR i Appendix C, Section V,
paragraph A, states that a notice of violation will generally not be issued
4
4
                            paragraph A, states that a notice of violation will generally not be issued
if a violation meets 5 stated criteria. This violation meets these criteria
                            if a violation meets 5 stated criteria. This violation meets these criteria
;
;                           and no notice of violation will be issued.
and no notice of violation will be issued.
,                            A permanent procedure to conduct the testing will also be written and
A permanent procedure to conduct the testing will also be written and
,
i
i
                            implemented by the MST rewrite group prior to the end of the next
implemented by the MST rewrite group prior to the end of the next
                            surveillance interval.
surveillance interval.
No violations or deviations were identified.
,
,
                            No violations or deviations were identified.
7.
                        7.  Operational Safety Verification (71707) (71710)
Operational Safety Verification (71707) (71710)
                            The inspectors verified conformance with regulatory requirements by direct
The inspectors verified conformance with regulatory requirements by direct
:                           observations of activities, facility tours, discussions with personnel,
:
                            reviewing of records and independent verification of safety system status.
observations of activities, facility tours, discussions with personnel,
                            The inspectors verified that control room manning requirements of 10 CFR
reviewing of records and independent verification of safety system status.
_
The inspectors verified that control room manning requirements of 10 CFR
                            50.54 and the Technical Specifications were met. Control room, shift
50.54 and the Technical Specifications were met.
Control room, shift
_
supervisor, clearance and jumper / bypass logs were reviewed to obtain
i
i
                            supervisor, clearance and jumper / bypass logs were reviewed to obtain
information concerning operating trends and out of service safety systems to
                            information concerning operating trends and out of service safety systems to
ensure that there were no conflicts with Technical Specifications Limiting
                            ensure that there were no conflicts with Technical Specifications Limiting
j
j                           Conditions for Operations. Direct observations wera conducted of control
Conditions for Operations.
Direct observations wera conducted of control
!
!
!
!
,
,
      - - - .               - - . +       - . ~ . , , - - , - - . .. s-. -.     ,,   ,a,.   . ~ . . , , . - , . , - , . ,.m   ,,-,r-+-. -, - - , , - , , -
- - - .
- - . +
- . ~ . , , - - , - - .
..
s-.
-.
,,
,a,.
. ~ . . ,
,
. - , . , - , .
,.m
,,-,r-+-.
-, - - , , - , , -


    . - - -                               -   _         _                       ._     .       .       .
. - - -
              .
-
  .
_
                                                        6
_
                .
._
                  room panels, instrumentation and recorder traces important to safety to
.
                  verify operability and that parameters were within Technical Specification
.
                  limits. The inspectors observed shift turnovers to verify that continuity
.
                  of system status was maintained.       The inspectors verified the status of
.
                  selected control room annunciators.
.
J                 Operability of a selected ESF train was verified by insuring that: each
6
;                 accessible valve in the flow path was in its correct position; each power
.
                  supply and breaker, including control room fuses, were aligned for
room panels, instrumentation and recorder traces important to safety to
,
verify operability and that parameters were within Technical Specification
                  components that must activate upon initiation signal; removal of power from
limits. The inspectors observed shift turnovers to verify that continuity
'
of system status was maintained.
                  those ESF motor-operated valves, so identified by Technical Specifications,
The inspectors verified the status of
                  was completed; there was no leakage of major components; there was proper
selected control room annunciators.
                  lubrication and cooling water available; and a condition did not exist which
J
                  might prevent fulfillment of the system's functional                 requirements.
Operability of a selected ESF train was verified by insuring that: each
                  Instrumentation essential to system actuation or performance was verified
;
                  operable by observing on-scale indication and proper instrument valve
accessible valve in the flow path was in its correct position; each power
                  lineup, if accessible.
supply and breaker, including control room fuses, were aligned for
                  The inspectors verified that the licensee's health physics policies / pro-
components that must activate upon initiation signal; removal of power from
                  cedures were followed. This included a review of             area surveys, radiation
,
those ESF motor-operated valves, so identified by Technical Specifications,
'
was completed; there was no leakage of major components; there was proper
lubrication and cooling water available; and a condition did not exist which
might prevent fulfillment of the system's functional
requirements.
Instrumentation essential to system actuation or performance was verified
operable by observing on-scale indication and proper instrument valve
lineup, if accessible.
The inspectors verified that the licensee's health physics policies / pro-
cedures were followed.
This included a review of area surveys, radiation
l
l
                  work permits, posting, and instrument calibration.
work permits, posting, and instrument calibration.
                  The inspectors verified that: the security organization was properly manned
The inspectors verified that: the security organization was properly manned
                  and that security personnel were cepable of performing their assigned
and that security personnel were cepable of performing their assigned
                  functions; persons and packages were checked prior to entry into the
functions; persons and packages were checked prior to entry into the
                  protected area (PA); vehicles were properly authorized, searched and
protected area (PA); vehicles were properly authorized, searched and
                  escorted within the PA; persons within the PA displayed photo identification
escorted within the PA; persons within the PA displayed photo identification
                  badges; personnel in vital areas were authorized; effective compensatory
badges; personnel in vital areas were authorized; effective compensatory
                  measures were employed when required; and security's response to threats or
measures were employed when required; and security's response to threats or
                  alarms was adequate.
alarms was adequate.
                  The inspectors also observed plant housekeeping controls, verified position
The inspectors also observed plant housekeeping controls, verified position
                  of certain containment isolation valves, checked clearances, and verified
of certain containment isolation valves, checked clearances, and verified
                  the operability of onsite and offsite emergency power sources.
the operability of onsite and offsite emergency power sources.
                  No violations or deviations were identified.
No violations or deviations were identified.
            8.   Onsite Review Committee (40700)
8.
                  The inspectors attended selected Plant Nuclear Safety Committee meetings                     '
Onsite Review Committee (40700)
                  conducted during the period. The inspectors verified that the meetings were
'
                  conducted in accordance with Technical Specification requirements regarding
The inspectors attended selected Plant Nuclear Safety Committee meetings
                  quorum membership, review process, frequency and personnel qualifications.
conducted during the period. The inspectors verified that the meetings were
                  No violations or deviations were identified.
conducted in accordance with Technical Specification requirements regarding
quorum membership, review process, frequency and personnel qualifications.
No violations or deviations were identified.
,
,
                                                                                                                i
i
!
!
                                                                    _ _ . _ _       _     _     _
_
                                                                                                      ..  _.
_
..
_.
_ _ . _ _
_


    _.     .-   -.             ..             -                                           . _ - .
_.
        .
.-
  .
-.
                                                7
..
        9. Onsite Review of Licensee Event Reports (92700)
-
          The listed Licensee Event Reports (LER's) were reviewed to verify that the
. _ - .
          information provided met NRC reporting requirements. The verification
.
          included adequacy of event description and corrective action taken or
.
          planned, existence of potential generic problems and the relative safety
7
          significance of the event. Onsite inspections were performed and concluded
9.
          that necessary corrective actions have been taken in accordance with
Onsite Review of Licensee Event Reports (92700)
          existing requirements, licensee conditions and commitments.   The following
The listed Licensee Event Reports (LER's) were reviewed to verify that the
          reports are considered closed:
information provided met NRC reporting requirements.
          (Closed) LER 1-80-20; Containment monitoring system isolated due -to
The verification
          personnel error.
included adequacy of event description and corrective action taken or
          (Closed) LER 1-81-34; Four supports were found damaged due to water hammer.
planned, existence of potential generic problems and the relative safety
          (Closed) LER 1-83-10; Fire barrier / secondary containment seal degradation
significance of the event. Onsite inspections were performed and concluded
          allows water to leak into reactor building.
that necessary corrective actions have been taken in accordance with
existing requirements, licensee conditions and commitments.
The following
reports are considered closed:
(Closed) LER 1-80-20; Containment monitoring system isolated due -to
personnel error.
(Closed) LER 1-81-34; Four supports were found damaged due to water hammer.
(Closed) LER 1-83-10; Fire barrier / secondary containment seal degradation
allows water to leak into reactor building.
,
,
          (Closed) LER 1-83-23; Fire in 4160/480 volt E-6 transformer.
(Closed) LER 1-83-23; Fire in 4160/480 volt E-6 transformer.
;         (Closed) LER 1-83-26; Diesel generator trips due to operator failing to
;
          follow procedure.
(Closed) LER 1-83-26; Diesel generator trips due to operator failing to
          (Closed) LER 1-83-32; Control rods have no position indication.
follow procedure.
          (Closed) LER 1-83-36; Control power fuse to motor operator blew due to
(Closed) LER 1-83-32; Control rods have no position indication.
          ground in circuit.
(Closed) LER 1-83-36; Control power fuse to motor operator blew due to
          (Closed) LER 1-83-40; Inadequate surveillance procedure and personnel error
ground in circuit.
(Closed) LER 1-83-40; Inadequate surveillance procedure and personnel error
cause HPCI to isolate.
,
,
          cause HPCI to isolate.
(Closed) LER 1-83-62; Reactor building exhaust ventilation radiation monitor
          (Closed) LER 1-83-62; Reactor building exhaust ventilation radiation monitor
actuated outside technical specification limit.
          actuated outside technical specification limit.
(Closed) LER 1-84-01; Air entrapped in suction header caused residual heat
          (Closed) LER 1-84-01; Air entrapped in suction header caused residual heat
removal service water pumps to trip.
          removal service water pumps to trip.
!
!         (Closed) LER 1-84-29; Spurious actuation of control building emergency air
(Closed) LER 1-84-29; Spurious actuation of control building emergency air
i          filtration system.
filtration system.
i
t
t
          (Closed) LER 1-84-30; Spurious actuation of control building emergency air
(Closed) LER 1-84-30; Spurious actuation of control building emergency air
          filtration system.
filtration system.
          (Closed) LER 1-84-31; Spurious actuation of control building emergency air               i
(Closed) LER 1-84-31; Spurious actuation of control building emergency air
          filtration system.
i
          (Closed) LER 1-85-02; Automatic isolation of the control building heating,               ;
filtration system.
          ventilation and air conditioning system due to spurious chlorine signal.                 l
(Closed) LER 1-85-02; Automatic isolation of the control building heating,
                                                                                                    1
ventilation and air conditioning system due to spurious chlorine signal.
                                                                                                    i
i
I
I
                                                  __
__
                                                                  -
-
                                                                              . _ _ . . _ ,
. _ _ . . _ ,


      .
.
  - .
- .
                                                                                      l
8
                                                                                      l
(Closed) LER 1-85-03; Inadequate logic system functional testing of degraded
                                            8
and under-voltage relays of emergency buses.
        (Closed) LER 1-85-03; Inadequate logic system functional testing of degraded
(Closed) LER 1-85-05; Inadequate functional testing of rod block monitor.
        and under-voltage relays of emergency buses.
(Closed) LER 1-85-07; Spurious actuation of control building emergency air
        (Closed) LER 1-85-05; Inadequate functional testing of rod block monitor.
filtration system.
        (Closed) LER 1-85-07; Spurious actuation of control building emergency air
(Closed) LER 1-85-14; Steam leak causes reactor core isolation cooling
        filtration system.
system isolation.
        (Closed) LER 1-85-14; Steam leak causes reactor core isolation cooling
(Closed) LER 1-85-17; Loss of emergency bus E-1 normal feed.
        system isolation.
(Closed) LER 1-35-19; Control building emergency air filtration system
        (Closed) LER 1-85-17; Loss of emergency bus E-1 normal feed.
actuation due to accidental shorting of detector circuit.
        (Closed) LER 1-35-19; Control building emergency air filtration system
(Closed) LER 1-85-22; Standby gas treatment train IA relay over heats and
        actuation due to accidental shorting of detector circuit.
fails.
        (Closed) LER 1-85-22; Standby gas treatment train IA relay over heats and
(Closed) LER 2-83-41; A " rod drift" annunciation was received due to the rod
        fails.
position indication probe.
        (Closed) LER 2-83-41; A " rod drift" annunciation was received due to the rod
(Closed) LER 2-83-46; Wires to terminals in the terminal box were reversed.
        position indication probe.
(Closed) LER 2-83-52; Transmitter shorted to ground when alligator clip test
        (Closed) LER 2-83-46; Wires to terminals in the terminal box were reversed.
leads were accidentally bumped.
        (Closed) LER 2-83-52; Transmitter shorted to ground when alligator clip test
(Closed) LER 2-83-62; Prima ry containment temperature exceeds technical
        leads were accidentally bumped.
specification limit as result of seasonal ambient temperatures.
        (Closed) LER 2-83-62; Prima ry containment temperature exceeds technical
(Closed) LER 2-83-65; Condensate storage tank level switches for High
        specification limit as result of seasonal ambient temperatures.
Pressure Coolant Injection (HPCI) system improperly installed.
        (Closed) LER 2-83-65; Condensate storage tank level switches for High
(Closed) LER 2-83-71; Suppression pool temperature exceeds limit as result
        Pressure Coolant Injection (HPCI) system improperly installed.
of HPCI run.
        (Closed) LER 2-83-71; Suppression pool temperature exceeds limit as result
(Closed) LER 2-83-82; Suppression pool level exceeds limit due to personnel
        of HPCI run.
error.
        (Closed) LER 2-83-82; Suppression pool level exceeds limit due to personnel
(Closed) LER 2-83-84.
        error.
This item was voided by the Licensee.
        (Closed) LER 2-83-84.   This item was voided by the Licensee.
(Closed) LER 2-83-94; Reed switch problems cause incorrect position
        (Closed) LER 2-83-94; Reed switch problems cause incorrect position
indication.
        indication.
(Closed) LER 2-84-04; Reactor scram initiated by HFA relay replacement and
        (Closed) LER 2-84-04; Reactor scram initiated by HFA relay replacement and
surveillance testing.
        surveillance testing.
[
[
'
'
        (Closed) LER 2-84-06; Procedure failed to identify the need for jumping the
(Closed) LER 2-84-06; Procedure failed to identify the need for jumping the
        low low level signal.
low low level signal.
:
:


    .                   __       . - _ _ _ .             .__ _ .                                     .                                 - __.                       _._
.
                      .
__
  .
. - _ _ _ .
      .
.__
_ .
.
- __.
_._
.
.
.
4
4
3
3
  i
i
                                                                                          9
9
:
:
4
4
                            (Closed) LER 2-85-01; Surveillance test not performed within allowable time
(Closed) LER 2-85-01; Surveillance test not performed within allowable time
                            due to inadvertent deletion from scheduling system.
due to inadvertent deletion from scheduling system.
                            (Closed) LER 2-85-03; Inadequate surveillance procedure results in an
(Closed) LER 2-85-03; Inadequate surveillance procedure results in an
                            unexpected group 1 isolation.
unexpected group 1 isolation.
;                          No violations or deviations were identified.
No violations or deviations were identified.
                      10. Refueling Activities (60710)
;
                            During the licensee's refueling operations, the inspectors verified that
10.
  i
Refueling Activities (60710)
                            selected surveillance testing required by Technical Specifications was
During the licensee's refueling operations, the inspectors verified that
!                           current and that the licensee's fuel- handling procedure was implemented.
i
'
selected surveillance testing required by Technical Specifications was
                            The following additional items were verified:
!
;
current and that the licensee's fuel- handling procedure was implemented.
                            a.   Selected fuel bundle movements,
'
                            b.   Core monitcring during refuel operations was in accordance with
The following additional items were verified:
                                Technical Specifications.
a.
                            c.   Vessel water level was maintained in accordance with Technical
Selected fuel bundle movements,
;
b.
Core monitcring during refuel operations was in accordance with
Technical Specifications.
c.
Vessel water level was maintained in accordance with Technical
Specification.
1
1
                                Specification.                                                                                                                          ,
i
                                                                                                                                                                        '
,
i
'
                            d.   Reactor mode switch position was as required by Technical Specifi-
d.
                                cation.
Reactor mode switch position was as required by Technical Specifi-
f
cation.
                            e.   Continuous communications were maintained between the refueling                                                                         ,
f
e.
Continuous communications were maintained between the refueling
,
platform and the control room and that . control room operators were
1
1
                                platform and the control room and that . control room operators were
cognizant of the applicable procedure steps.
                                cognizant of the applicable procedure steps.
f.
                            f.   Health-Physics personnel maintained constant coverage of all fuel
Health-Physics personnel maintained constant coverage of all fuel
j                               moving activities, ensuring area dose rates, contamination levels and
j
                                airborne samples were within required tolerances.
moving activities, ensuring area dose rates, contamination levels and
                            No violations or deviations were identified.
airborne samples were within required tolerances.
                      11. Modification Process and Masonry Walls (37700)                                                                                               i
No violations or deviations were identified.
)                                                                                                                                                                       i
11. Modification Process and Masonry Walls (37700)
                            During review of design activities, the inspector reviewed the licensee's
i
'
)
i
'
During review of design activities, the inspector reviewed the licensee's
method for ensuring that safety related equipment would not be installed on
-
-
                            method for ensuring that safety related equipment would not be installed on
j-
j-                         or in close proximity to masonry walls whose failure could affect the
or in close proximity to masonry walls whose failure could affect the
equipment (Bulletin 80-11 concern).
The method currently employed relies
+
+
                            equipment (Bulletin 80-11 concern).                                    The method currently employed relies
upon -notes on the wall drawings to inform the user of the wall status
                            upon -notes on the wall drawings to inform the user of the wall status
(analyzed or unanalyzed) and their general engineering practice of. not
                            (analyzed or unanalyzed) and their general engineering practice of. not
installing new supports onto masonry walls.
                            installing new supports onto masonry walls.                                     These appear to adequately
These appear to adequately
                            address installation onto walls but do not provide a positive means to
address installation onto walls but do not provide a positive means to
j                           ensure that safety related equipment is not placed close to an unanalyzed
j
ensure that safety related equipment is not placed close to an unanalyzed
!
!
i
i
l
l
I
I
        ,, + - ~ - - -       .,               , , - - - -         ,w., ,-n-- , , - - - . . -----n,.     ~e-- , .,,,,.,..p o-m-,,--m.v w w. ,. mg-m m.- --.,--,,,. ,,e
,, + - ~ - - -
.,
, , - - - -
,w.,
,-n--
, , - - - . .
-----n,.
~e--
,
.,,,,.,..p
o-m-,,--m.v
w w.
,.
mg-m m.-
--.,--,,,. ,,e


  .
.
.
                                        10
.
    wall (walls which did not have safety related equipment around them were not
10
    analyzed per Bulletin 80-11).       This is an inspector followup item
wall (walls which did not have safety related equipment around them were not
    (324/85-27-03 and 325/85-27-03): Enhancements of controls to preclude
analyzed per Bulletin 80-11).
    installation of safety related equipment in proximity to unanalyzed masonry
This is an inspector followup item
    walls.
(324/85-27-03 and 325/85-27-03): Enhancements of controls to preclude
    No violations or deviations were identified.
installation of safety related equipment in proximity to unanalyzed masonry
walls.
No violations or deviations were identified.
}}
}}

Latest revision as of 23:47, 24 May 2025

Insp Repts 50-324/85-27 & 50-325/85-27 on 850801-31. Violation Noted:Bolts Replaced on Hydraulic Control Units W/Type Other than Specified on Drawings
ML20137X384
Person / Time
Site: Brunswick  Duke Energy icon.png
Issue date: 09/20/1985
From: Fredrickson P, Garner L, Hicks T
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML20137X354 List:
References
50-324-85-27, 50-325-85-27, NUDOCS 8510040510
Download: ML20137X384 (11)


See also: IR 05000324/1985027

Text

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pn Rico

UNITED STATES

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NUCLEAR REGULATORY COMMISSION

et' *$ k

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REGION 11

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101 MARIETTA STREET. N.W.

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ATLANTA, GEORGI A 30323

% .' ,',#

SEP 2 31985

,.

Report Nos. 50-325/85-27 and 50-324/85-27

Licensee: Carolina Power and Light Company

P. O. Box 1551

Raleigh, NC 27602

1

Docket Nos.:

50-325 and 50-324

License Nos.

DPR-71 and DPR-62

Facility Name: Brunswick 1 and 2

Inspection Co

ed:

ugust 1 ; 31,1985

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Inspectors:

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Vate figned

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Approved By:

-

P. E. Fredrickson, Section Chief

Dite Signed

Division of Reactor Projects

SUMMARY

Scope: This routine safety inspection involved 177 inspector-hours on site in

the areas of maintenance observation, surveillance observation, operational

safety verification, onsite review committee, ESF System walkdown, Licensee Event

Reports review, follewup on inspector identified items, refueling activities and

plant modifications.

Results:

One violation was identified:

Bolts Replaced on Hydraulic Control

Units with Type Other Than That Specified on Drawings. One unresolved item was

identified:

Seismic Qualification of Hydraulic Control Unit Frame.

I

h0040510850923

G

ADOCK 05000324

PDR

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1

i

REPORT DETAILS

!

1.

Licensee Employees

Persons Contacted

,

P. Howe, Vice President - Brunswick Nuclear Project

.

C. Dietz, General Manager - Brunswick Nuclear Project

T. Wyllie, Manager - Engineering and Construction

,

G. Oliver, Manager - Site Planning and Control

!

J. Holder, Manager - Outages

l

E. Bishop, Assistant to General Manager

I

i

L. Jones, Director - QA/QC

r

M. Shealy, Acting Director - Training

,

M. Jones, Acting Director - Onsite Nuclear Safety - BSEP

J. Chase, Manager - Operations

'

J. O'Sullivan, Manager - Maintenance

G. Cheatham, Manager - Environmental & Radiation Control

,

4

K. Enzor, Director - Regulatory Compliance

B. Hinkley, Manager - Technical Support

L. Boyer, Director - Administrative Support

V. Wagoner, Director - IPBS/Long Range Planning

L

C. Blackmon, Superintendent - Operations

j

J. Wilcox, Principle Engineer - Operations

W. Hogle, Engineering Supervisor

W. Tucker, Engineering Supervisor

,

B. Wilson, Engineering Supervisor

R. Creech, I&C/ Electrical Maintenance Supervisor (Unit 2)

J. Moyer, I&C/ Electrical Maintenance Supervisor (Unit 1)

R. Kitchen, Mechanical Maintenance Supervisor (Unit 2)

R. Poulk, Senior.NRC Regulatory Specialist

D. Novotny, Senior Regulatory Specialist

W. Dorman, QA - Supervisor

4

W. Hatcher, Security Supervisor

.

W. Murray, Senior Engineer - Nuclear Licensing Unit

Other licensee employees contacted included construction craftsmen,

engineers, technicians, operators, office personnel, and security force

members.

,

!

2.

Exit Interview (30703)

i

The inspection scope and findings were summarized on September 5, 1985 with

the general manager.

The licensee acknowledged the findings without

i

exception.

The licensee did not identify as proprietary any of the

j

materials provided to or reviewed by the inspectors during the inspection.

3.

Followup on' Previous Enforcement Matters (92702)

Not inspected.

.

. - _ . . . - ,

- ..

.

- - . - - -

. . _ - . , ,

. . - . -

- _ - , , . - - - - . ,- ,,.-.-,.

_

..

.

a

2

i

4.

Followup on Inspector Followup Items

a.

(Closed) Inspector Followup Item 325, 324/84-35-02; Post Trip Reviews

01-22. An open item was generated after a reactor scram in December

1984 because of a questionable post trip review.

The item was to

follow the licensee's progress toward enhancing the scram review

process.

Revisions 8-10 to the Post Trip Review Procedure 01-22 were

the result of this effort.

These revisions clarify the responsibili-

ties of the operations engineer and other associated requirements.

This item is considered closed.

b.

(Closed)

Inspector

Followup

Item

324/84-31-03;

Standby Air

Compressors.

This item was opened because of a concern over the

inoperability of an automatic start pressure switch for a standby air

compressor.

The licensee has failed to find a suitable replacement,

I

but is presently undertaking a plant modification on Unit 1 (and is

planned on Unit 2) which will alleviate the need for these air

compressors during post accident conditions.

The modification will

install a nitrogen backup system which will supply the necessary

.

pneumatic pressure during accident conditions. This item is considered

!

closed.

I

c.

(Closed) Inspector Followup Item 325, 324/85-03-01; Radwas*e Shipping.

This item was generated to track improvements in the radwaste shipping

,

quality control program and the auditing of this program. This item is

considered closed because a notice of violation 325, 324/85-17-01 was

written in this area and will track corrective actions.

5.

Maintenance Observation (62703)

The inspectors observed maintenance activities and reviewed records to

verify that work was conducted in accordance with approved procedures,

Technical Specifications, and applicable industry codes and standards. The

inspectors also verified that:

redundant components were operable;

j

administrative controls were followed; tagouts were adequate; personnel were

qualified; correct replacement parts were used; radiological controls were

,

proper; fire protection was adequate; QC hold points were adequate and

observed; adequate post-maintenance testing was performed; and independent

verification requirements were implemented.

The inspectors independently

verified that selected equipment was properly returned to service.

4

Outstanding work requests and authorizations (WR&A) were reviewed to ensure

that the licensee gave priority to safety-related maintenance.

a.

Bolting Replacement and Seismic Qualification of Hydraulic Contr^1

Units

Inspection Report 325/85-22- issued a notice of violation for loose

<

and/or missing rack-support-to-foundation bolting for the control rod

!

hydraulic control units (HCU).

During followup of the repair and

replacement, it was observed by the inspector that all the replaced

i

i

_

,

_

_ _ - , _ _ , _ _ _

_____

,_. _

.

.

3

!

!

bolts (five) had been replaced with bolts which were not cadmium plated

as required by plant design drawing G.E. 919D615.

The apparent root

cause was that the maintenance planner verified that Q bolting was

,

required but failed to check the specifications for any special

requirements.

Discussion with licensee personnel indicates that this

may have been a common practice when replacing bolting. The licensee

is currently evaluating the impact of this on plant equipment.

Failure to install the type of bolting specified on G.E. 9190615

drawing is a violation of 10 CFR 50, Appendix

B,

Criterion V

(324/85-27-01):

Bolts Replaced on Hydraulic Control Units with Type

Other than that Specified on Drawings.

The licensee has attempted to establish the seismic qualification of

the as-found conditions documented in inspection report 325/85-22,

i.e., one HCU had 2 out of the 4 rack-support-to-foundation bolts

missing. Calculations were performed on the HCU's with missing bolts,

on HCU's which stand alone and on HCU's installed back-to-back with all

fasteners properly installed. The calculations show the as found HCU's

with loose or missing bolts met at least short term criteria (IEB 79-14),

i.e.,

bolts might deform but would not break.

The same

conclusion was deterrrined for the stand alone HCU's. However, in all

cases including back-to-back installation, stresses were calculated

which exceeded the allowable stress in the tubular frame. The original

i

seismic qualification was performed by the vendor (G.E.) based upon

results of field tests with the units tested back-to-back. This field

test data is not available to the licensee at this time. Without field

test data, the complexity of the installed configuration requires

several conservative assumptions to be made to allow analytic modeling.

The licensee believes that their calculated results are conservative.

Therefore, since the frame was qualified by the vendor from experi-

mental data, the licensee believes the frames to be qualified and the

HCU's are operable, i.e. seismically qualified. However, the licensee

expects to resolve this apparent discrepancy between their analytic

model and the original seismic qualification based on field data.

Resolution of this apparent discrepancy is an unresolved item

1

(325/85-27-01 and 324/85-27-02):

Seismic Qualification of HCU Frame,

b.

Post Maintenance Test Requirement Test Sheet Fails to Specify Pressure

Test /VT-2 Inspection

During a routine inspection of post maintenance surveillance testing

,

'

for the Unit I standby liquid control injection check valve C41-F007,

the inspector noticed that no pressure test /VT-2 inspection was

specified on the Post Maintenance Test Requirement (PMTR) sheet even

though the pressure boundary for the valve had been broken during

maintenance. The valve is Class 1.

Two similar maiatenance activities

4

involving Class 1 valves B21-F028B and B21-F019 were also reviewed and

found to not contain the pressure test /VT-2 inspection requirement on

i

'

4

- - - . ,

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_ -

_ _ _

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-- . _ = - -

-

. _ _ - - _ _

- - - .

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.

.

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.

4

the PMTR sheet. It became clear that the maintenance planners were not

using ENP-16, Inservice Inspection Requirements, properly.

After

scoping the jobs and realizing that the work involved disassembly of

the valves, the planners should have realized that the pressure

boundaries of each of these valves was to be broken and that entry into

Section VI, Visual Inspection, of ENP-16 was necessary to determine

additional post maintenance test requirements.

This process was not

done.

,

i

The problem was discussed with plant management and the following

!

immediate corrective actions were taken:

(1) Training was conducted for all mechanical maintenance planners in

'

the proper use of ENP-16.

(2) A review was conducted of PMTR's for Class 1 valves worked during

the Unit 1 outage.

For those which required pressure test /VT-2

inspections, an additional test / inspection was included on the

PMTR sheet. Those activities already closed out, were reopened by

an additional PMTR sheet stating the required test.

At the completion of the present Unit 1 outage, a vessel

hydrostatic test and inspection including all Class 1 piping and

components is to be performed (PT-80.1, 10 year Inservice

Inspection Reactor Vessel Hydrostatic Test). This test would have

satisfied the inservice inspection requirements for the valves

identified. Followup of long term corrective actions will be an

-

inspector followup

item (IFI 325/85-27-02): Administrative

!.

Control Changes to Ensure Pressure Test /VT-2 Inspections are

Identified as Post Maintenance Requirements.

f

6.

Surveillance Observation (61726)

l

)

The inspectors observed surveillance testing required by Technical

Specifications.

Through observation and record review, the inspectors

verified that:

tests conformed to Technical Specification requirements;

administrative

controls were

followed;

personnel

were

qualified;

instrumentation was calibrated; and data was accurate and complete.

The

inspectors independently verified selected test results and proper return to

4

service of equipment.

A special review was performed of the following Licensee finding:

On August 21, 1985, the Maintenance Surveillance Test (MST) rewrite group

discovered that Periodic Tests, PT-A22.2-1,

PT-22.2-2,

PT-A24.2 and

PT-45.2.4, covering Secondary Containment Isolation Response Time Testing,

did not adequately test all the relays in the associated logic circuit.

,

Technical Specification Surveillance 4.3.2.3 requires that this be done

'

every 18 months.

i

,

-

, , - .

,_

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_

_ _ _ _

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.

-

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.

,

.

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4

.

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5

,

Specifically, relays K66, K67, 3AA, 3AB, 3BA, 3BB, 3BD, A-CRMX and B-CRMX

,/

were not being included in the response time test. At the time, Unit I was

shutdown for a refueling outage (no core alterations were in progress) and

Unit 2 was at 100% power.

The surveillance test problem involved both

>

units.

4

Licensee management conducted a Plant Nuclear Safety Committee (PNSC)

meeting concerning this problem and concluded that there was no technical

reason to consider this instrumentation inoperable based on the following:

,

a.

Relays not presently being timed have been verified operable in logic

4

system functional tests which were performed in October 1984 (Unit 2).

b.

The manufacturer's expected response time for these relays is less than

85 milliseconds.

c.

The allowed response time for the instrumentation is less than or equal

to 13 seconds.

Adding the relay's expected response time to the

existing instrumentation response time still results in a response time

of less than or equal to 1 second.

A special test procedure was generated to test the relays (SP-85-086) and

'was satisfactorily performed for Units i and 2 on August 25, 1985.

,

These inadequate procedures constitute a violation of Technical Specifi-

i.

cation Surveillance 4.3.2.3,.in that they failed to adequately response time

1,

test all the necessary relays. However,10 CFR i Appendix C,Section V,

paragraph A, states that a notice of violation will generally not be issued

4

if a violation meets 5 stated criteria. This violation meets these criteria

and no notice of violation will be issued.

A permanent procedure to conduct the testing will also be written and

,

i

implemented by the MST rewrite group prior to the end of the next

surveillance interval.

No violations or deviations were identified.

,

7.

Operational Safety Verification (71707) (71710)

The inspectors verified conformance with regulatory requirements by direct

observations of activities, facility tours, discussions with personnel,

reviewing of records and independent verification of safety system status.

The inspectors verified that control room manning requirements of 10 CFR 50.54 and the Technical Specifications were met.

Control room, shift

_

supervisor, clearance and jumper / bypass logs were reviewed to obtain

i

information concerning operating trends and out of service safety systems to

ensure that there were no conflicts with Technical Specifications Limiting

j

Conditions for Operations.

Direct observations wera conducted of control

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room panels, instrumentation and recorder traces important to safety to

verify operability and that parameters were within Technical Specification

limits. The inspectors observed shift turnovers to verify that continuity

of system status was maintained.

The inspectors verified the status of

selected control room annunciators.

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Operability of a selected ESF train was verified by insuring that: each

accessible valve in the flow path was in its correct position; each power

supply and breaker, including control room fuses, were aligned for

components that must activate upon initiation signal; removal of power from

,

those ESF motor-operated valves, so identified by Technical Specifications,

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was completed; there was no leakage of major components; there was proper

lubrication and cooling water available; and a condition did not exist which

might prevent fulfillment of the system's functional

requirements.

Instrumentation essential to system actuation or performance was verified

operable by observing on-scale indication and proper instrument valve

lineup, if accessible.

The inspectors verified that the licensee's health physics policies / pro-

cedures were followed.

This included a review of area surveys, radiation

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work permits, posting, and instrument calibration.

The inspectors verified that: the security organization was properly manned

and that security personnel were cepable of performing their assigned

functions; persons and packages were checked prior to entry into the

protected area (PA); vehicles were properly authorized, searched and

escorted within the PA; persons within the PA displayed photo identification

badges; personnel in vital areas were authorized; effective compensatory

measures were employed when required; and security's response to threats or

alarms was adequate.

The inspectors also observed plant housekeeping controls, verified position

of certain containment isolation valves, checked clearances, and verified

the operability of onsite and offsite emergency power sources.

No violations or deviations were identified.

8.

Onsite Review Committee (40700)

'

The inspectors attended selected Plant Nuclear Safety Committee meetings

conducted during the period. The inspectors verified that the meetings were

conducted in accordance with Technical Specification requirements regarding

quorum membership, review process, frequency and personnel qualifications.

No violations or deviations were identified.

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9.

Onsite Review of Licensee Event Reports (92700)

The listed Licensee Event Reports (LER's) were reviewed to verify that the

information provided met NRC reporting requirements.

The verification

included adequacy of event description and corrective action taken or

planned, existence of potential generic problems and the relative safety

significance of the event. Onsite inspections were performed and concluded

that necessary corrective actions have been taken in accordance with

existing requirements, licensee conditions and commitments.

The following

reports are considered closed:

(Closed) LER 1-80-20; Containment monitoring system isolated due -to

personnel error.

(Closed) LER 1-81-34; Four supports were found damaged due to water hammer.

(Closed) LER 1-83-10; Fire barrier / secondary containment seal degradation

allows water to leak into reactor building.

,

(Closed) LER 1-83-23; Fire in 4160/480 volt E-6 transformer.

(Closed) LER 1-83-26; Diesel generator trips due to operator failing to

follow procedure.

(Closed) LER 1-83-32; Control rods have no position indication.

(Closed) LER 1-83-36; Control power fuse to motor operator blew due to

ground in circuit.

(Closed) LER 1-83-40; Inadequate surveillance procedure and personnel error

cause HPCI to isolate.

,

(Closed) LER 1-83-62; Reactor building exhaust ventilation radiation monitor

actuated outside technical specification limit.

(Closed) LER 1-84-01; Air entrapped in suction header caused residual heat

removal service water pumps to trip.

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(Closed) LER 1-84-29; Spurious actuation of control building emergency air

filtration system.

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(Closed) LER 1-84-30; Spurious actuation of control building emergency air

filtration system.

(Closed) LER 1-84-31; Spurious actuation of control building emergency air

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filtration system.

(Closed) LER 1-85-02; Automatic isolation of the control building heating,

ventilation and air conditioning system due to spurious chlorine signal.

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(Closed) LER 1-85-03; Inadequate logic system functional testing of degraded

and under-voltage relays of emergency buses.

(Closed) LER 1-85-05; Inadequate functional testing of rod block monitor.

(Closed) LER 1-85-07; Spurious actuation of control building emergency air

filtration system.

(Closed) LER 1-85-14; Steam leak causes reactor core isolation cooling

system isolation.

(Closed) LER 1-85-17; Loss of emergency bus E-1 normal feed.

(Closed) LER 1-35-19; Control building emergency air filtration system

actuation due to accidental shorting of detector circuit.

(Closed) LER 1-85-22; Standby gas treatment train IA relay over heats and

fails.

(Closed) LER 2-83-41; A " rod drift" annunciation was received due to the rod

position indication probe.

(Closed) LER 2-83-46; Wires to terminals in the terminal box were reversed.

(Closed) LER 2-83-52; Transmitter shorted to ground when alligator clip test

leads were accidentally bumped.

(Closed) LER 2-83-62; Prima ry containment temperature exceeds technical

specification limit as result of seasonal ambient temperatures.

(Closed) LER 2-83-65; Condensate storage tank level switches for High

Pressure Coolant Injection (HPCI) system improperly installed.

(Closed) LER 2-83-71; Suppression pool temperature exceeds limit as result

of HPCI run.

(Closed) LER 2-83-82; Suppression pool level exceeds limit due to personnel

error.

(Closed) LER 2-83-84.

This item was voided by the Licensee.

(Closed) LER 2-83-94; Reed switch problems cause incorrect position

indication.

(Closed) LER 2-84-04; Reactor scram initiated by HFA relay replacement and

surveillance testing.

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(Closed) LER 2-84-06; Procedure failed to identify the need for jumping the

low low level signal.

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(Closed) LER 2-85-01; Surveillance test not performed within allowable time

due to inadvertent deletion from scheduling system.

(Closed) LER 2-85-03; Inadequate surveillance procedure results in an

unexpected group 1 isolation.

No violations or deviations were identified.

10.

Refueling Activities (60710)

During the licensee's refueling operations, the inspectors verified that

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selected surveillance testing required by Technical Specifications was

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current and that the licensee's fuel- handling procedure was implemented.

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The following additional items were verified:

a.

Selected fuel bundle movements,

b.

Core monitcring during refuel operations was in accordance with

Technical Specifications.

c.

Vessel water level was maintained in accordance with Technical

Specification.

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d.

Reactor mode switch position was as required by Technical Specifi-

cation.

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Continuous communications were maintained between the refueling

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platform and the control room and that . control room operators were

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cognizant of the applicable procedure steps.

f.

Health-Physics personnel maintained constant coverage of all fuel

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moving activities, ensuring area dose rates, contamination levels and

airborne samples were within required tolerances.

No violations or deviations were identified.

11. Modification Process and Masonry Walls (37700)

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During review of design activities, the inspector reviewed the licensee's

method for ensuring that safety related equipment would not be installed on

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or in close proximity to masonry walls whose failure could affect the

equipment (Bulletin 80-11 concern).

The method currently employed relies

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upon -notes on the wall drawings to inform the user of the wall status

(analyzed or unanalyzed) and their general engineering practice of. not

installing new supports onto masonry walls.

These appear to adequately

address installation onto walls but do not provide a positive means to

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ensure that safety related equipment is not placed close to an unanalyzed

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wall (walls which did not have safety related equipment around them were not

analyzed per Bulletin 80-11).

This is an inspector followup item

(324/85-27-03 and 325/85-27-03): Enhancements of controls to preclude

installation of safety related equipment in proximity to unanalyzed masonry

walls.

No violations or deviations were identified.