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                        U.S. NJCLEAR REGULATORY COMMISSION
U.S. NJCLEAR REGULATORY COMMISSION
                                      REGION III
REGION III
                Docket Nos:       50-10: 50-237: 50-249
Docket Nos:
                License Nos:-     DPR-2: DPR-19: DPR-25
50-10: 50-237: 50-249
              .
License Nos:-
                Report No:         50-010/96014: 50-237/96014 50-249/96014
DPR-2: DPR-19: DPR-25
                Licensee:         Commonwealth Edison Company
.
                Facility:         Dresden Nuclear Station Units 1. 2 and 3
Report No:
l               Location:         Opus West III
50-010/96014: 50-237/96014 50-249/96014
,                                  1400 Opus Place - Suite 300
Licensee:
l                                  Downers Grove. IL 60515
Commonwealth Edison Company
Facility:
Dresden Nuclear Station Units 1. 2 and 3
l
Location:
Opus West III
1400 Opus Place - Suite 300
,
,
                Dates:           October 21 through December 6. 1996
l
                Inspectors:     C. Vanderniet. Senior Resident Inspector
Downers Grove. IL 60515
,
Dates:
October 21 through December 6. 1996
Inspectors:
C. Vanderniet. Senior Resident Inspector
.
.
J. Hansen. Resident Inspector
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                                  J. Hansen. Resident Inspector
D. Roth. Resident Inspector
                                  D. Roth. Resident Inspector
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C. Settles. Inspe tor. Illinois Department of
I
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                                  C. Settles. Inspe tor. Illinois Department of
Nuclear Sa ety
                                  Nuclear Sa ety
FAI'
                Approved By:
Approved By:
                                  FAI'
P. L. Hiland. Chief
                                  P. L. Hiland. Chief
Reactor Projects Branch 1
                                  Reactor Projects Branch 1
9702100277 970204
      9702100277 970204
PDR
      PDR ADOCK 05000010
ADOCK 05000010
      G               PDR
G
PDR


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!                                     EXECUTIVE SUMMARY
!
                          Dresden Nuclear Station Units 1. 2 and 3
EXECUTIVE SUMMARY
              iiRC Inspection Report 50-10/96014: 50-237/96014: 50-249/96014
Dresden Nuclear Station Units 1. 2 and 3
      This routine resident inspection included aspects of licensee operations.
iiRC Inspection Report 50-10/96014: 50-237/96014: 50-249/96014
      maintenance, engineering, and plant support. The report covered a 7-week
This routine resident inspection included aspects of licensee operations.
      period of resident inspection.
maintenance, engineering, and plant support.
      Doerations
The report covered a 7-week
      .    The facility was operated in a safe manner and previously identified
period of resident inspection.
            minor deficiencies were corrected (Section 01.1).
Doerations
      .    The Unit 3 low pressure heater bay had improved accessibility and
The facility was operated in a safe manner and previously identified
            housekeeping; however, minor material deficiencies were identified by
.
            the inspectors (Section 01.2).
minor deficiencies were corrected (Section 01.1).
      .    A manual reactor trip was initiated in response to a loss of the 3B
The Unit 3 low pressure heater bay had improved accessibility and
            reactor recirculation motor generator set. Plant and safety equipment
.
            functioned as expected (Section 02.1).
housekeeping; however, minor material deficiencies were identified by
      .    Unit 3 emergency diesel generator (EDG) ejected a cylinder test valve
the inspectors (Section 01.2).
            after a surveillance run. No personnel injuries or significant damage
A manual reactor trip was initiated in response to a loss of the 3B
            resulted and after minor repairs the EDG was returned to service
.
            (Section 02.2).
reactor recirculation motor generator set.
      Maintenance
Plant and safety equipment
      .    In general, maintenance activities were well controlled: however, two
functioned as expected (Section 02.1).
            work stoppages were issued due to non-safety related parts control and
Unit 3 emergency diesel generator (EDG) ejected a cylinder test valve
            contractor work practices (Section M1.1).
.
                                                                                    l
after a surveillance run.
      .    Significant repair work on the 3B reactor recirculation pump motor was   l
No personnel injuries or significant damage
            well executed and managed. Root cause for the motor failure was foreign !
resulted and after minor repairs the EDG was returned to service
            material intrusion into the stator windings (Section M2.1).             l
(Section 02.2).
      .    Construction era rag was found inside the Unit 3 high pressure coolant
Maintenance
            injection (HPCI) lube oil cooler waterbox. Tube leaks were repaired and
In general, maintenance activities were well controlled: however, two
            the system was restored to service (Section M2.2).
.
      Enoineerina
work stoppages were issued due to non-safety related parts control and
      .    The licensee failed to perform post-modification testing on the Unit 2/3
contractor work practices (Section M1.1).
            main control room heating, ventilation and air conditioning (HVAC)
l
            system. This was an apparent violation (Section E2.1).                   l
Significant repair work on the 3B reactor recirculation pump motor was
      .    An engineer failed to enter vendor technical information into the vendor
.
            equipment technical information program (VETIP) as required by plant     l
well executed and managed.
            procedures (Section E4.1).
Root cause for the motor failure was foreign
                                              2
material intrusion into the stator windings (Section M2.1).
l
Construction era rag was found inside the Unit 3 high pressure coolant
.
injection (HPCI) lube oil cooler waterbox.
Tube leaks were repaired and
the system was restored to service (Section M2.2).
Enoineerina
The licensee failed to perform post-modification testing on the Unit 2/3
.
main control room heating, ventilation and air conditioning (HVAC)
system. This was an apparent violation (Section E2.1).
An engineer failed to enter vendor technical information into the vendor
.
equipment technical information program (VETIP) as required by plant
procedures (Section E4.1).
2


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      .
Ins)ector review of two tem)orary alterations identified some problems
            Ins)ector review of two tem)orary alterations identified some problems
.
            wit 1 implementation and tecinical evaluation (Section E4.2).
,
                                                                                      ,
wit 1 implementation and tecinical evaluation (Section E4.2).
                                                                                      l
Plant Support
      Plant Support
Computer accounting system failed at the beginning of the plant assembly
                                                                                      l
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                                                                                      !
drill causing confusion. A thorough drill critique identified
      .
deficiencies and corrective actions (Section P4.1).
            Computer accounting system failed at the beginning of the plant assembly
Problems were identified with the level indication and switch
            drill causing confusion. A thorough drill critique identified
.
            deficiencies and corrective actions (Section P4.1).
calibration on the Unit 1 diesel-driven fire pump (Section F2.1).
      .
'
            Problems were identified with the level indication and switch
            calibration on the Unit 1 diesel-driven fire pump (Section F2.1).       '
                                                                                      1
                                                                                      l
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1
1
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3
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                                      REPORT DETAILS
REPORT DETAILS
    Summary of Plant Status
Summary of Plant Status
          Unit 2 began the period at a reduced load of about 300 MWe as some
Unit 2 began the period at a reduced load of about 300 MWe as some
          maintenance activities were concluded. The unit was returned to full
maintenance activities were concluded. The unit was returned to full
          power on October 22.   On October 27 a 2% power derate was initiated due
power on October 22.
          to feedwater flow instrument uncertainty. On November 23 a load drop
On October 27 a 2% power derate was initiated due
          was made to facilitate a drywell entry to add oil to the 2A reactor
to feedwater flow instrument uncertainty. On November 23 a load drop
          recirculation pump motor. The unit was returned to near full power the
was made to facilitate a drywell entry to add oil to the 2A reactor
          following day. On November 26 the 2% derate was lifted and the unit
recirculation pump motor. The unit was returned to near full power the
          returned to full power. On November 28. power was reducea for changing
following day.
          condensate demineralizes and exercising control rod drives. The unit     :
On November 26 the 2% derate was lifted and the unit
          began a slow power increase on December 2 and returned to full power on
returned to full power. On November 28. power was reducea for changing
          December 3.
condensate demineralizes and exercising control rod drives.
          Unit 3 commenced this inspection period in coastdown in preparation for
The unit
          refueling outage D3R14. On October 26. the 3B motor generator (MG) set
:
          tripped and after a short period of single loop operations the reactor
began a slow power increase on December 2 and returned to full power on
          was manually tripped on October 27. and a forced outage commenced.
December 3.
                                      I. OPERATIONS
Unit 3 commenced this inspection period in coastdown in preparation for
    01   Conduct of Operations
refueling outage D3R14. On October 26. the 3B motor generator (MG) set
    01.1 General Comments (71707)
tripped and after a short period of single loop operations the reactor
          Routine day-to-day facility operations were observed by inspectors both
was manually tripped on October 27. and a forced outage commenced.
          in the control room and in the field. Main control board walkdowns and
I. OPERATIONS
          reviews of various operating logs were also performed. Previous           l
01
          observations discussed in Inspection Re) ort 50-237/249-96013. dated
Conduct of Operations
          December 31. 1996 regarding minor breacdowns in control room decorum.     l
01.1 General Comments (71707)
          3-way communications, and responsiveness to annunciators were not
Routine day-to-day facility operations were observed by inspectors both
          observed during this inspection period. Generally, operator performance
in the control room and in the field.
          inside the control room continued to be crisp and professional. A
Main control board walkdowns and
          weakness was noted with operations personnel outside the control room.   1
reviews of various operating logs were also performed.
          specifically, operator knowledge of the Unit 1 diesel-driven fire pump   ;
Previous
          day tank level switches (paragraph F2.1).
observations discussed in Inspection Re) ort 50-237/249-96013. dated
    01.2 Tour of Low Pressure Heater Bay (Unit 3)
December 31. 1996 regarding minor breacdowns in control room decorum.
      a. Insoection Scone (71707)
3-way communications, and responsiveness to annunciators were not
          The inspectors toured Unit 3 low 3ressure heater bay and observed the
observed during this inspection period. Generally, operator performance
          general material condition houseceeping, and temporary alterations
inside the control room continued to be crisp and professional. A
          installed on heater drain valves.
weakness was noted with operations personnel outside the control room.
      b. Observations and Findinos
1
          Overall the inspectors noted significantly improved housekeeping over
specifically, operator knowledge of the Unit 1 diesel-driven fire pump
          the past nine months; however, numerous undocumented material
day tank level switches (paragraph F2.1).
          discrepancies were identified. These discrepancies included valves
01.2 Tour of Low Pressure Heater Bay (Unit 3)
                                              4
a.
Insoection Scone (71707)
The inspectors toured Unit 3 low 3ressure heater bay and observed the
general material condition houseceeping, and temporary alterations
installed on heater drain valves.
b.
Observations and Findinos
Overall
the inspectors noted significantly improved housekeeping over
the past nine months; however, numerous undocumented material
discrepancies were identified.
These discrepancies included valves
4


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            missing packing gland fasteners. open junction and electrical cable pull
missing packing gland fasteners. open junction and electrical cable pull
            boxes. and misadjusted piping hangers. After a discussion about general
boxes. and misadjusted piping hangers.
            conditions, several items were identified to the licensee for
After a discussion about general
            correction.
conditions, several items were identified to the licensee for
            Followup tours of the Unit 3 LP heater bay found that the specific items
correction.
            had been addressed and a few additional items had been identified by the
Followup tours of the Unit 3 LP heater bay found that the specific items
            licensee. One of the additional items identified by the licensee was an
had been addressed and a few additional items had been identified by the
            o)en lighting junction box above one of the room exits. The tag for
licensee.
            t11s item was attached to a cable tray protective cover through a hole
One of the additional items identified by the licensee was an
            where the cover bolt and stud had broken off. Additionally. the cover
o)en lighting junction box above one of the room exits. The tag for
            had several loose or broken nuts, however, none of these deficiencies     l
t11s item was attached to a cable tray protective cover through a hole
            were identified by the licensee.                                         l
where the cover bolt and stud had broken off. Additionally. the cover
        c. Conclusions
had several loose or broken nuts, however, none of these deficiencies
            The significant improvement in the housekeeping of the LP heater bay
were identified by the licensee.
            allowed a greater portion of the room to be more easily accessible. The
c.
            reduction in contaminated areas further improved accessibility to the
Conclusions
            room.   However, the identification of material condition problems in
The significant improvement in the housekeeping of the LP heater bay
            less traveled areas of the plant continued to be a challenge.
allowed a greater portion of the room to be more easily accessible.
      02   Operational Status of Facilities and Equipment
The
      02.1 Recirculation Motor-Generator (MG) Set "B" Trio (Unit 3)
reduction in contaminated areas further improved accessibility to the
                                                                                      1
room.
        a. Insoection Stone (71707)
However, the identification of material condition problems in
            On October 26. at 1758 the 3B Recirculation pump tripped due to tri) ping
less traveled areas of the plant continued to be a challenge.
            of the 3B MG set. Onsite response to this event was performed by t1e
02
            inspectors, and observation of control room personnel performance during
Operational Status of Facilities and Equipment
            the power reduction and manual reactor scram was accomplished.   The
02.1 Recirculation Motor-Generator (MG) Set "B" Trio (Unit 3)
            following operational procedures were reviewed:
a.
            .
Insoection Stone (71707)
                  Dresden Annunciator Procedure (DAN) 903-4 A6. 3B RECIRC M-G SET
On October 26. at 1758 the 3B Recirculation pump tripped due to tri) ping
                  GEN LOCKOUT.
of the 3B MG set.
            .
Onsite response to this event was performed by t1e
                  DAN 903-4 A7. 3B RECIRC PP DP LO.
inspectors, and observation of control room personnel performance during
            .     DAN 903-4 08, 3B RECIRC PP LOWER LUBE OIL LVL LO.
the power reduction and manual reactor scram was accomplished.
            .
The
                  Dresden Operating Abnormal (DOA) 0202-01. Recirculation Pump Trip
following operational procedures were reviewed:
                  One or Both Pumps.
Dresden Annunciator Procedure (DAN) 903-4 A6. 3B RECIRC M-G SET
            .
.
                  Dresden General Procedure (DGP) 02-01. Unit 2 (3) NORMAL UNIT
GEN LOCKOUT.
                  SHUTDOWN
DAN 903-4 A7. 3B RECIRC PP DP LO.
            .      DGP 02-03. REACTOR SCRAM
.
            .     DGP 03-03. SINGLE RECIRCULATION LOOP OPERATION
DAN 903-4 08, 3B RECIRC PP LOWER LUBE OIL LVL LO.
        b. Observations and Findinos
.
Dresden Operating Abnormal (DOA) 0202-01. Recirculation Pump Trip
.
One or Both Pumps.
Dresden General Procedure (DGP) 02-01. Unit 2 (3) NORMAL UNIT
.
SHUTDOWN
DGP 02-03. REACTOR SCRAM
.
DGP 03-03. SINGLE RECIRCULATION LOOP OPERATION
.
b.
Observations and Findinos
l
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l           The root cause of the MG set trip was not immediately known and single   1
l
l          loop operation commenced. The inspectors responded to the site and       i
The root cause of the MG set trip was not immediately known and single
            monitored the reactor down power and the subsequent manual reactor trip   I
loop operation commenced.
            at 0201 on October 27. After the 3B MG set tripped, the 3A MG set was
The inspectors responded to the site and
            reduced to 60 percent power in accordance with approved procedures and
l
                                              5
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monitored the reactor down power and the subsequent manual reactor trip
at 0201 on October 27. After the 3B MG set tripped, the 3A MG set was
reduced to 60 percent power in accordance with approved procedures and
5
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Line 220: Line 272:
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          the unit was stabilized at about 34 percent power. Power was further
.
          decreased to 25 percent using recirculation flow and a manual reactor
the unit was stabilized at about 34 percent power.
          trip signal initiated.   Systems responded as expected with the exception
Power was further
          of rod position indication failures for two rods and two intermediate
decreased to 25 percent using recirculation flow and a manual reactor
          range monitor failures. For the evolutions observed plant operators
trip signal initiated.
          followed all appropriate procedures during the course of the shutdown.
Systems responded as expected with the exception
          Control room decorum and 3-way communications were maintained throughout
of rod position indication failures for two rods and two intermediate
          the event.
range monitor failures.
      c. Conclusion
For the evolutions observed plant operators
          The plant response to the loss of a single reactor recirculation pump
followed all appropriate procedures during the course of the shutdown.
          was in accordance with expectations and plant design. The control room
Control room decorum and 3-way communications were maintained throughout
          operators followed procedures and conducted an orderly shutdown.
the event.
    02.2 Emergency Diesel Generator (EDG) E.iected a Cylinder Test Valve Durina
c.
          Troubleshootina Run (Unit 3)
Conclusion
      a. Inspection Scone (71707)
The plant response to the loss of a single reactor recirculation pump
          The inspectors observed a test of the Unit 3 EDG and observed the
was in accordance with expectations and plant design.
          licensee's response to the observed test failure. Field observations,
The control room
          system and equipment inspection walkdowns were performed before and
operators followed procedures and conducted an orderly shutdown.
          after the valve ejection occurred.     Additionally, the inspectors
02.2 Emergency Diesel Generator (EDG) E.iected a Cylinder Test Valve Durina
          reviewed the following documentation
Troubleshootina Run (Unit 3)
                                                                                    l
a.
          .      Vendor Equipment Technical Information Program (VETIP) Manual
Inspection Scone (71707)
                  1163. Electro-Motive Diesel Engine.
The inspectors observed a test of the Unit 3 EDG and observed the
          .
licensee's response to the observed test failure.
                  Dresden Electrical Surveillance (DTS) 6600-01. Diesel Generator
Field observations,
                  Governor Oil Change and Compensation Adjustment
system and equipment inspection walkdowns were performed before and
          .      Dresden Operations Surveillance (DOS) 6600-01. " Diesel Generator
after the valve ejection occurred.
                  Surveillance Test."
Additionally, the inspectors
      b. Observations and Findinas
reviewed the following documentation
          On November 24. the inspectors observed performance of Dresden
Vendor Equipment Technical Information Program (VETIP) Manual
          Electrical Surveillance (DTS) 6600-01 for the Unit 3 EDG. No
.
          abnormalities were noted during the initial performance of the test.
1163. Electro-Motive Diesel Engine.
          Subsequent to test performance, the Shift Manager informed the
Dresden Electrical Surveillance (DTS) 6600-01. Diesel Generator
          inspectors that the EDG had ejected a cylinder test valve from
.
          Cylinder 20. The High Voltage Operator (HVO) had entered the room to
Governor Oil Change and Compensation Adjustment
          secure the EDG and reported that the test valve had blown out. The
Dresden Operations Surveillance (DOS) 6600-01. " Diesel Generator
          inspectors returned to the Unit 3 EDG room shortly after the EDG was
.
          secured.
Surveillance Test."
                                                                                    I
b.
          The test valve had blown out of Cylinder 20 on the EDG generator end.
Observations and Findinas
          The valve appeared to have impacted the wall directly adjacent to the
On November 24. the inspectors observed performance of Dresden
          valve and fallen to the floor. No damage was evident from the valve
Electrical Surveillance (DTS) 6600-01 for the Unit 3 EDG.
          ejection, other than carbon buildup on piping near the cylinder test
No
          valve port. Inspection of the test valve showed no damage or unusual
abnormalities were noted during the initial performance of the test.
          wear. No personnel injuries were reported and the licensee immediately     i
Subsequent to test performance, the Shift Manager informed the
          initiated a prompt investigation into the event.                         )
inspectors that the EDG had ejected a cylinder test valve from
                                                                                    ,
Cylinder 20.
The High Voltage Operator (HVO) had entered the room to
secure the EDG and reported that the test valve had blown out.
The
inspectors returned to the Unit 3 EDG room shortly after the EDG was
secured.
I
The test valve had blown out of Cylinder 20 on the EDG generator end.
The valve appeared to have impacted the wall directly adjacent to the
valve and fallen to the floor.
No damage was evident from the valve
ejection, other than carbon buildup on piping near the cylinder test
valve port.
Inspection of the test valve showed no damage or unusual
wear.
No personnel injuries were reported and the licensee immediately
i
initiated a prompt investigation into the event.
)
,


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l                                                                                                .
l        During additional inspection on November 25. the inspectors noted that
          the Unit 3 EDG cylinder test valves did not appear to be threaded into                i
                                                                                                1
l        the cylinder block as far as the test valves on the Unit 2 or 2/3 EDGs.                1
          This information was conveyed to the licensee's team performing the                    !
          prompt event investigation.
l        The prompt investigation c termined that the test valves had been                      j
          replaced in December 1995, and that the ejected valve must have had a                  ,
          relaxed torque that was further loosened due to normal EDG vibrations.                '
          Additionally. Cylinder 20 on the Unit 3 EDG was the cylinder with the
          highest compression pressure on the engine. The licensee did not
          perform a formal root cause evaluation of this event although several
          corrective actions were performed. The EDG was repaired and was                        i
          returned to service on November 27.
      c. Conclusions
          Operations personnel performed the surveillance testing in accordance
          with the appropriate procedures and were observed closely monitoring EDG
          performance.
    08    Miscellaneous Operations Issues (92700)
    08.1  (Closed) Violation (50-237:249/95010-03): Control of Overtime Not
          Implemented In Accordance With Generic Letter (GL) 82-12. Revision 1 to
          Dresden Operating Procedure 01-09. Control of Overtime authorized
          November 14, 1995, incorporated the guidance established in GL 82-12.
          This action appeared adequate to prevent recurrence: however, the
          recently completed independent safety inspection (ref. IR 50-237:249/96-
          201, dated December 24, 1996. Section 6.3.3) identified continuing
          problems with corrective action for control of overtime. This item is
          closed and further followup will be documented against Independent
          Safety Inspection (ISI) Deficiency 50-237:249/96-201-29
    08.2 (Closed) Insoector Followuo item (IFI) 50-237:249/96002-04:    Atmospheric
          Containment Atmosphere Dilution (ACAD) Operating and Surveillance
          Procedures' Bands Differ. The inspectors noted that the ACAD system air
          receiver operating pressure band was being maintained at 44 to 57 psig,
          which was above the band in Dresden Operating Procedure (DOP) 2500-01.
          "ACAD Dilution Subsystem Operation" (41 to 52 psig). Dresden Operating
          Surveillance (DOS) 2500-01. "ACAD Compressor Surveillance," and Dresden
          Administrative Technical Requirements (DATR) both listed a pressure band
          of 44 to 57 psig. To resolve this issue, the licensee planned to revise
          the appropriate ACAD procedures. The inspector reviewed the revised
          ACAD procedure (DOP 2500-01) and the changes to the UFSAR and had no
          further concerns. This item is closed.
l
l
l
l
l                                             7
l
During additional inspection on November 25. the inspectors noted that
.
the Unit 3 EDG cylinder test valves did not appear to be threaded into
1
the cylinder block as far as the test valves on the Unit 2 or 2/3 EDGs.
l
1
This information was conveyed to the licensee's team performing the
!
prompt event investigation.
l
The prompt investigation c termined that the test valves had been
j
replaced in December 1995, and that the ejected valve must have had a
,
relaxed torque that was further loosened due to normal EDG vibrations.
'
Additionally. Cylinder 20 on the Unit 3 EDG was the cylinder with the
highest compression pressure on the engine. The licensee did not
perform a formal root cause evaluation of this event although several
corrective actions were performed.
The EDG was repaired and was
i
returned to service on November 27.
c.
Conclusions
Operations personnel performed the surveillance testing in accordance
with the appropriate procedures and were observed closely monitoring EDG
performance.
08
Miscellaneous Operations Issues (92700)
08.1
(Closed) Violation (50-237:249/95010-03):
Control of Overtime Not
Implemented In Accordance With Generic Letter (GL) 82-12.
Revision 1 to
Dresden Operating Procedure 01-09. Control of Overtime authorized
November 14, 1995, incorporated the guidance established in GL 82-12.
This action appeared adequate to prevent recurrence: however, the
recently completed independent safety inspection (ref. IR 50-237:249/96-
201, dated December 24, 1996. Section 6.3.3) identified continuing
problems with corrective action for control of overtime. This item is
closed and further followup will be documented against Independent
Safety Inspection (ISI) Deficiency 50-237:249/96-201-29
08.2 (Closed) Insoector Followuo item (IFI) 50-237:249/96002-04:
Atmospheric
Containment Atmosphere Dilution (ACAD) Operating and Surveillance
Procedures' Bands Differ. The inspectors noted that the ACAD system air
receiver operating pressure band was being maintained at 44 to 57 psig,
which was above the band in Dresden Operating Procedure (DOP) 2500-01.
"ACAD Dilution Subsystem Operation" (41 to 52 psig).
Dresden Operating
Surveillance (DOS) 2500-01. "ACAD Compressor Surveillance," and Dresden
Administrative Technical Requirements (DATR) both listed a pressure band
of 44 to 57 psig.
To resolve this issue, the licensee planned to revise
the appropriate ACAD procedures.
The inspector reviewed the revised
ACAD procedure (DOP 2500-01) and the changes to the UFSAR and had no
further concerns. This item is closed.
l
l
l
7


    -
-
  .
.
l                                                                                    1
l
l
1
l
II. Maintenance
'
'
                                        II. Maintenance
M1
                                                                                      1
Conduct of Haintenance
      M1    Conduct of Haintenance                                                   l
l
                                                                                      1
M1.1 General Comments (62707)
,
,
      M1.1 General Comments (62707)
'
'
            In general, maintenance activities at the facility were well controlled   1
In general, maintenance activities at the facility were well controlled
                                                                                      l
and performed in accordance with approved work packages and procedures.
            and performed in accordance with approved work packages and procedures.   1
Numerous tasks were observed in the field and minor observations were
            Numerous tasks were observed in the field and minor observations were     i
discussed with the appropriate licensee staff.
            discussed with the appropriate licensee staff. Scheduling and work
Scheduling and work
            planning continued to be difficult 3roblems. This was evident when a
planning continued to be difficult 3roblems.
            stop work order was issued during t1e conduct of maintenance which left
This was evident when a
            an oil pump for both the 2A and 2B MG set oil skids out of service,
stop work order was issued during t1e conduct of maintenance which left
            thereby leaving both MG sets in a more vulnerable condition.             i
an oil pump for both the 2A and 2B MG set oil skids out of service,
            Significant work activities that were performed during this inspection   .
thereby leaving both MG sets in a more vulnerable condition.
            period not receiving specific comment included the following;             l
Significant work activities that were performed during this inspection
            .      3D Electromatic Relief Valve Flange Leak Repair
.
            .     Unit 3 EDG Power Pack Replacement
period not receiving specific comment included the following;
            Additionally, during this report period the licensee issued two stop
3D Electromatic Relief Valve Flange Leak Repair
            work orders. The first, issued November 21. regarded the retraining of   l
.
            contractor personnel in the use of nuclear standard work procedures.     i
Unit 3 EDG Power Pack Replacement
            This was in response to a failure of contract worker personnel to comply l
.
            with facility safe work practices. The second, issued November 24
Additionally, during this report period the licensee issued two stop
            regarded the procurement and use of non-safety related parts. This was
work orders. The first, issued November 21. regarded the retraining of
            partially in response to the 3A control rod drive pump discharge
contractor personnel in the use of nuclear standard work procedures.
            isolation valve that was installed with a through wall pinhole leak.
i
            Both work stoppages were of short duration and were appropriate
This was in response to a failure of contract worker personnel to comply
            resomses to address specific maintenance problems.
with facility safe work practices. The second, issued November 24
      H2   Maintenance Material Condition of Facility and Equipment
regarded the procurement and use of non-safety related parts.
      M2.1 "B" Reactor Recirculation (RR) Pumo Motor Repair (Unit 3)
This was
        a. Inspection Scope (62707)
partially in response to the 3A control rod drive pump discharge
            During the report period, the inspectors observed licensee actions to
isolation valve that was installed with a through wall pinhole leak.
            troubleshoot and repair the 3B reactor recirculation (RR) motor trip.
Both work stoppages were of short duration and were appropriate
            Portions of the field preparation and actual repair were observed by the
resomses to address specific maintenance problems.
            inspectors. In addition, work package preparation and s3ecial rigging
H2
            and load testing documentation were reviewed including t1e following:
Maintenance Material Condition of Facility and Equipment
            .      Vendor Manual GEK-26132. " Boiling Water Nuclear Reactor
M2.1
                  Recirculating Water Pump Motors for the Dresden 11 and III nuclear
"B" Reactor Recirculation (RR) Pumo Motor Repair (Unit 3)
                  power station of the Commonwealth Edison Company by the General
a.
                  Electric Atomic Power Equipment Department."
Inspection Scope (62707)
            .      Special Procedure (SP) 96-11-019. "3B RR Pump Motor In-place
During the report period, the inspectors observed licensee actions to
                  Repair."
troubleshoot and repair the 3B reactor recirculation (RR) motor trip.
Portions of the field preparation and actual repair were observed by the
inspectors.
In addition, work package preparation and s3ecial rigging
and load testing documentation were reviewed including t1e following:
Vendor Manual GEK-26132. " Boiling Water Nuclear Reactor
.
Recirculating Water Pump Motors for the Dresden 11 and III nuclear
power station of the Commonwealth Edison Company by the General
Electric Atomic Power Equipment Department."
Special Procedure (SP) 96-11-019. "3B RR Pump Motor In-place
.
Repair."
,
,
                                                8
8


  -
-
.
.
      *      Dresden Engineering Document 5254777. " Reactor Recirculation Pump
Dresden Engineering Document 5254777. " Reactor Recirculation Pump
              Motor Refurbishment - Details for the Engineered Impact Mat -
*
              Unit 3."
Motor Refurbishment - Details for the Engineered Impact Mat -
      .      Dresden Engineering Document 5257492. " Reactor Recirculation Pump
Unit 3."
              Motor Refurbishment - Details for Pump Bowl Shimming. Engineered
Dresden Engineering Document 5257492. " Reactor Recirculation Pump
              Impact Mat and Rigging."
.
      .      Dresden Engineering Document 5253222. " Rigging of the 3B Recir.
Motor Refurbishment - Details for Pump Bowl Shimming. Engineered
              Pump Motor End Bell. Rotor and Stator to Repair the Motor in
Impact Mat and Rigging."
              Place."
Dresden Engineering Document 5253222. " Rigging of the 3B Recir.
    b. Observations and Findinas
.
      After the October 26, 3B RR pump MG set trip. the licensee's               ,
Pump Motor End Bell. Rotor and Stator to Repair the Motor in
      troubleshooting effort located a ground in the pump motor. Two             l
Place."
      approaches to resolve the problem were developed; repair the motor in-     '
b.
      place, or replacement with a rebuilt motor. A rebuilt motor was
Observations and Findinas
      obtained and brought to the site, but work to repair in-place continued.
After the October 26, 3B RR pump MG set trip. the licensee's
      The repair work included load-testing the drywell monorail: design.       l
,
      testing, and installation of an engineered impact mat: development of a   !
troubleshooting effort located a ground in the pump motor. Two
      rigging plan for the motor endbell, rotor and stator; and identifying     j
approaches to resolve the problem were developed; repair the motor in-
      possible repair techniques. The plan called for the removal of the         !
'
      motor endbell and rotor and the lifting of the stator. The stator
place, or replacement with a rebuilt motor. A rebuilt motor was
      needed to be lifted high enough to allow access for inspection and         !
obtained and brought to the site, but work to repair in-place continued.
      repair. Once the package was finally prepared, a special )lant             !
The repair work included load-testing the drywell monorail: design.
      operations review committee (PORC) reviewed and approved t1e plan.         !
testing, and installation of an engineered impact mat: development of a
      During the preparation of the work, the inspectors reviewed selected
rigging plan for the motor endbell, rotor and stator; and identifying
      portions of the packages and observed monorail and impact mat testing.     j
j
      The use of a computer-generated animation of the lifting process greatly   1
possible repair techniques. The plan called for the removal of the
      aided all personnel in understanding the job. Also, the assignment of
motor endbell and rotor and the lifting of the stator.
      the Operations Manager as a dedicated project manager ensured continuity
The stator
      on the project.
needed to be lifted high enough to allow access for inspection and
      During the stator inspection a small piece of banding material was
repair.
      discovered shorting one motor phase. The foreign material was removed
Once the package was finally prepared, a special )lant
      and the damaged area of the windings repaired. After successfully
operations review committee (PORC) reviewed and approved t1e plan.
      testing the windings, the motor was reassembled. The piece of banding     ,
During the preparation of the work, the inspectors reviewed selected
      material most likely entered the motor in late 1990 to early 1991 time     l
portions of the packages and observed monorail and impact mat testing.
      frame when the endbell had been removed for maintenance. The banding
j
      material was similar to material used to secure component identification
The use of a computer-generated animation of the lifting process greatly
      label plates inside the drywell. The licensee suspected that some of
aided all personnel in understanding the job. Also, the assignment of
      this material was dropped into the motor and eventually shorted the
the Operations Manager as a dedicated project manager ensured continuity
      stator. Additional foreign material found inside the motor was removed.
on the project.
      The intrusion of foreign material into various components at the
During the stator inspection a small piece of banding material was
      facility has been a longstanding problem. However, the inspectors'
discovered shorting one motor phase. The foreign material was removed
      recent observations of foreign material exclusion (ME) practices
and the damaged area of the windings repaired. After successfully
      indicated that significant improvements have been made over past
testing the windings, the motor was reassembled.
      practices.
The piece of banding
                                          9
,
material most likely entered the motor in late 1990 to early 1991 time
frame when the endbell had been removed for maintenance. The banding
material was similar to material used to secure component identification
label plates inside the drywell. The licensee suspected that some of
this material was dropped into the motor and eventually shorted the
stator.
Additional foreign material found inside the motor was removed.
The intrusion of foreign material into various components at the
facility has been a longstanding problem.
However, the inspectors'
recent observations of foreign material exclusion (ME) practices
indicated that significant improvements have been made over past
practices.
9


                                    _
_
    -
-
  .
.
l
l
          The ins)ectors observed various activities as the work progressed and
The ins)ectors observed various activities as the work progressed and
          noted tlat the job was well managed and skillfully performed.
noted tlat the job was well managed and skillfully performed.
          Disassembly, re) air. and reassembly progressed as expected and no major
Disassembly, re) air. and reassembly progressed as expected and no major
          problems with t1e work plans were encountered. Radiation protection
problems with t1e work plans were encountered.
          controls and practices were followed and the use of a video monitor for
Radiation protection
t          the viewing of the work was a good "as low as reasonably achievable"
controls and practices were followed and the use of a video monitor for
l         (ALARA) practice.
the viewing of the work was a good "as low as reasonably achievable"
      c. Conclusions
t
          The 3B RR pump motor repair was well coordinated.     Management and Site
l
          Quality Verification oversight were maintained and no significant
(ALARA) practice.
!         unanticipated problems occurred. The finding of several pieces of
c.
          foreign material inside a major component was not a new issue at the
Conclusions
          facility and efforts to improve FME continued to receive appropriate
The 3B RR pump motor repair was well coordinated.
          management attention.
Management and Site
      M2.2 Rao Found in Hiah Pressure Coolant Iniection (HPCI) Lube Oil Cooler.
Quality Verification oversight were maintained and no significant
            (Unit 2)
!
      a. Inspection Scone (62707)
unanticipated problems occurred. The finding of several pieces of
          The inspectors ins)ected the Unit 2 HPCI lube oil cooler and observed
foreign material inside a major component was not a new issue at the
          the rag found by t1e licensee during emergent maintenance work. A
facility and efforts to improve FME continued to receive appropriate
          review of the licensee's efforts to identify when the rag entered the
management attention.
          system was also performed,
M2.2 Rao Found in Hiah Pressure Coolant Iniection (HPCI) Lube Oil Cooler.
      b. Observations and Findinas                                                   !
(Unit 2)
          The HPCI system was declared inoperable on November 27. due to excessive   l
a.
          water contamination in the turbine lubricating oil. While performing       i
Inspection Scone (62707)
          maintenance to repair the water leaks in the lube oil cooler,
The inspectors ins)ected the Unit 2 HPCI lube oil cooler and observed
          maintenance personnel discovered a rag in the cooler water box. The rag
the rag found by t1e licensee during emergent maintenance work. A
          covered a significant portion of the cooler tube openings and appeared
review of the licensee's efforts to identify when the rag entered the
          to have been acting as a filter for the cooling medium.
system was also performed,
          The licensee suspects that the rag had been used as an FME cover during
b.
          facility construction and was never removed. The assumption was
Observations and Findinas
          substantiated due to the lack of finding any previous maintenance items
The HPCI system was declared inoperable on November 27. due to excessive
          that required removal of the HPCI lube oil cooler endbells in the
l
          maintenance database.     Further database searches showed that no recorded
water contamination in the turbine lubricating oil.
          maintenance work had been performed on the cooler or cooling system that
While performing
          would have allowed visual identification of the rag since the system was
i
          originally placed in service. The licensee also reviewed surveillance
maintenance to repair the water leaks in the lube oil cooler,
          test data and did not identify any instance of the HPCI system being
maintenance personnel discovered a rag in the cooler water box. The rag
          inoperable or degraded due to inadequate lube oil cooler performance.
covered a significant portion of the cooler tube openings and appeared
          Repair efforts were completed and the cooler was reassembled and
to have been acting as a filter for the cooling medium.
          satisfactorily tested.     Unit 2 HPCI was returned to service on
The licensee suspects that the rag had been used as an FME cover during
          December 1, with no further problems.
facility construction and was never removed.
                                              10
The assumption was
substantiated due to the lack of finding any previous maintenance items
that required removal of the HPCI lube oil cooler endbells in the
maintenance database.
Further database searches showed that no recorded
maintenance work had been performed on the cooler or cooling system that
would have allowed visual identification of the rag since the system was
originally placed in service. The licensee also reviewed surveillance
test data and did not identify any instance of the HPCI system being
inoperable or degraded due to inadequate lube oil cooler performance.
Repair efforts were completed and the cooler was reassembled and
satisfactorily tested.
Unit 2 HPCI was returned to service on
December 1, with no further problems.
10
.
-


.____m         . . . _ _     ._. _ _ _ _ _ _ _ . _ _ _ _                           . _ _ _ _ . _ _ _ . _
.____m
      -
. . . _ _
.   .
._. _ _ _ _ _ _ _ . _ _ _ _
. _ _ _ _ . _ _ _ . _
-
.
.
0
0
1
1
!
!
            c.       Conclusions
c.
Conclusions
:
:
i-                   All observed maintenance activities were performed in a skilled manner,
i-
All observed maintenance activities were performed in a skilled manner,
i
however, the discovery of the rag in the cooler further emphasized the
i
i
                    however, the discovery of the rag in the cooler further emphasized the
need to continue monitoring FME controls.
i                    need to continue monitoring FME controls.
;
;
            -
-
                                                                                                          I
Miscellaneous Maintenance Issues (92902)
        M8          Miscellaneous Maintenance Issues (92902)                                             I
M8
i       M8.1         (Closed) Insoector Followuo Item 50-237/249-95008-01: Failure to Follow
i
                    Procedure Resulted in Two Inoperable Core Spray Systems. On April 24,               '
M8.1
                    1995, the licensee reused o-rings on environmentally qualified equipment             l
(Closed) Insoector Followuo Item 50-237/249-95008-01:
}                   and only hand tightened the transmitter covers in violation of the                   l
Failure to Follow
Procedure Resulted in Two Inoperable Core Spray Systems.
On April 24,
'
1995, the licensee reused o-rings on environmentally qualified equipment
}
and only hand tightened the transmitter covers in violation of the
3rocedure. The inspectors reviewed information on reused o-rings and
)
*
*
                      3rocedure. The inspectors reviewed information on reused o-rings and                )
.
.
                      land tightened covers in CHRON # 0308805 and a referenced letter from               '
land tightened covers in CHRON # 0308805 and a referenced letter from
i                   Rosemount. The information a)peared adequate to support the licensee's
'
l                   operability determination. T11s item is closed.
i
Rosemount.
The information a)peared adequate to support the licensee's
l
operability determination. T11s item is closed.
a
a
:
:
                                                          III. Enaineerina
III. Enaineerina
        E2         Engineering Support of Facilities and Equipment
E2
        E2.1 Failure to Perform Adeouate Post-Modification Testina of the Control
Engineering Support of Facilities and Equipment
                    Room Heatina and Air Conditionina (HVAC) System (Units 1. 2 and 3)
E2.1 Failure to Perform Adeouate Post-Modification Testina of the Control
            a.       Insoection Scope (37551)
Room Heatina and Air Conditionina (HVAC) System (Units 1. 2 and 3)
                    The inspectors continued to observe and monitor the licensee's progress
a.
                      in correcting control room HVAC design and testing deficiencies. The
Insoection Scope (37551)
                      following documentation was reviewed:
The inspectors continued to observe and monitor the licensee's progress
                    .
in correcting control room HVAC design and testing deficiencies.
                            Modifications M12-2/3-82-1. M12-0-87-005 and M12-0-86-006: Unit 1
The
                            Control Room Modifications.
following documentation was reviewed:
                      *      DTS 5750-06, " Control Room Standby HVAC Air Filtration Unit, and
Modifications M12-2/3-82-1. M12-0-87-005 and M12-0-86-006:
                            Refrigeration Condensing Unit Performance Requirements," dated
Unit 1
                            August 24, 1996.
.
            b.       Observations and Findinas
Control Room Modifications.
                    The licensee continued work on sealing penetrations into the Unit 2/3
DTS 5750-06, " Control Room Standby HVAC Air Filtration Unit, and
                    control room, auxiliary computer room, and train "B" HVAC rcom. At the
*
                      close of this report period, efforts to remove a temporary alteration
Refrigeration Condensing Unit Performance Requirements," dated
                      and return the auxiliary computer roo.n into the control room envelope
August 24, 1996.
                    were unsuccessful. The licensee continued testing and achieved and
b.
                    maintained positive pressure requirements with the exception of the
Observations and Findinas
                      auxiliary computer room. Further work was planned to correct problems
The licensee continued work on sealing penetrations into the Unit 2/3
                      in the computer room and return the room to the control room envelope.
control room, auxiliary computer room, and train "B" HVAC rcom.
                      Background information on this issue can be found in Inspection Report
At the
                      96013 (paragraph E2.4) and Independent Safety Inspection (ISI) Report
close of this report period, efforts to remove a temporary alteration
                      96-201 (paragraph 4.6.4.1). The significance of this event was
and return the auxiliary computer roo.n into the control room envelope
                      previously considered an Unresolved Item (50-237:249/95013-02).
were unsuccessful.
                                                                  11                                     ;
The licensee continued testing and achieved and
                                                                                                          I
maintained positive pressure requirements with the exception of the
auxiliary computer room.
Further work was planned to correct problems
in the computer room and return the room to the control room envelope.
Background information on this issue can be found in Inspection Report
96013 (paragraph E2.4) and Independent Safety Inspection (ISI) Report
96-201 (paragraph 4.6.4.1).
The significance of this event was
previously considered an Unresolved Item (50-237:249/95013-02).
11
I


  -
.
.
    c. ISI Report 96-201. dated December 24. 1997. Daragraoh 4.6.4.1
-
      Sections 6.4.2 and 9.4-3 of the UFSAR described the design basis for the
c.
      control room HVAC system. Section 6.4.2.4 stated that potential adverse
ISI Report 96-201. dated December 24. 1997. Daragraoh 4.6.4.1
      interactions between the control room emergency zone and adjacent zones
Sections 6.4.2 and 9.4-3 of the UFSAR described the design basis for the
      that may allow the transfer of toxic or radioactive gases into the
control room HVAC system.
      control room were minimized by maintaining the control room at a           ,
Section 6.4.2.4 stated that potential adverse
      positive pressure of 1/8-inch water gauge (iwg) during emergency           l
interactions between the control room emergency zone and adjacent zones
      pressurization modes, and with respect to adjacent areas.
that may allow the transfer of toxic or radioactive gases into the
      On October 8. 1996, the licensee declared the control room HVAC system
control room were minimized by maintaining the control room at a
      inoperable because of the inability to maintain the control room at a
positive pressure of 1/8-inch water gauge (iwg) during emergency
      positive pressure during normal operations and at 1/8 iwg with respect
,
      to the surrounding areas in the emergency mode.   The control room
pressurization modes, and with respect to adjacent areas.
      ventilation system had not been maintained or properly tested 'o ensure
On October 8. 1996, the licensee declared the control room HVAC system
      that the system operated within its design basis. Modifications had
inoperable because of the inability to maintain the control room at a
      been implemented, or partially implemented, which resulted in negative
positive pressure during normal operations and at 1/8 iwg with respect
      pressure within the control room and the inability to pressurize the     l
to the surrounding areas in the emergency mode.
      control room to 1/8 iwg in the emergency mode. In addition,
The control room
      instrumentation that was used to verify the control room pressure was
ventilation system had not been maintained or properly tested 'o ensure
      positive in the emergency mode had not been calibrated, and had not been
that the system operated within its design basis.
      installed in accordance with the piping and instrumentation diagram.       j
Modifications had
                                                                                  i
been implemented, or partially implemented, which resulted in negative
      In September 1996, the licensee began reviewirg open modifications for   '
l
      the control room ventilation system, and subsequently determined that
pressure within the control room and the inability to pressurize the
      several control room modifications, which had not been completed,         i
control room to 1/8 iwg in the emergency mode.
      contributed to the inability to pressurize the control room as stated in
In addition,
      the UFSAR.     These incomplete modifications were identified as a result ,
instrumentation that was used to verify the control room pressure was
      of the licensee's efforts to close all modifications or approve the as-   I
positive in the emergency mode had not been calibrated, and had not been
      built configuration. The specific modifications affecting the control
installed in accordance with the piping and instrumentation diagram.
      room included:
j
      .
i
              M12-0-87-005-D provided for the installation of security equipment
In September 1996, the licensee began reviewirg open modifications for
              such as bullet resistant plating for walls and ceilings, new east- l
'
                                                                                3
the control room ventilation system, and subsequently determined that
              west kitchen and locker room area fire and non-fire rated doors.   I
several control room modifications, which had not been completed,
              and the sealing of new and unused wall and floor penetrations.
i
              Field work was initiated in August 1991 and completed in           j
contributed to the inability to pressurize the control room as stated in
              January 1992. Post-modification testina was not oerformed.
the UFSAR.
                                                                                  !
These incomplete modifications were identified as a result
                                                                                l
,
      .      M12-0-87-005-E provided supply and exhaust ventilation systems for i
of the licensee's efforts to close all modifications or approve the as-
              the new locker room and kitchen areas, new fire dampers in duct
I
              work penetrating fire walls, control logic for operation of the
built configuration.
              isolation dampers, and an interlock for the exhaust fans from the
The specific modifications affecting the control
              isolation dampers. Field work was started in September 1991 and   l
room included:
              completed by June 1993. The oost-modification testina, includina
M12-0-87-005-D provided for the installation of security equipment
              loaic testina and emergency oressurization testina to verify
.
              1/8 iwa was not oerformed.
such as bullet resistant plating for walls and ceilings, new east-
      .      M12-0-86-006-C provided supply and return side duct silencers,     j
3
              thermally insulated duct work, and manual volume dampers in the
west kitchen and locker room area fire and non-fire rated doors.
                                                                                  :
I
                                          12
and the sealing of new and unused wall and floor penetrations.
                                                                                  i
Field work was initiated in August 1991 and completed in
j
January 1992.
Post-modification testina was not oerformed.
l
M12-0-87-005-E provided supply and exhaust ventilation systems for
i
.
the new locker room and kitchen areas, new fire dampers in duct
work penetrating fire walls, control logic for operation of the
isolation dampers, and an interlock for the exhaust fans from the
isolation dampers.
Field work was started in September 1991 and
l
completed by June 1993. The oost-modification testina, includina
loaic testina and emergency oressurization testina to verify
1/8 iwa was not oerformed.
M12-0-86-006-C provided supply and return side duct silencers,
j
.
thermally insulated duct work, and manual volume dampers in the
:
12
i


'
'
    '                                                                               1
'
  .
j
                                                                                  j
.
                                                                                    1
shared return duct works.
                                                                                    l
The field work was started in
                                                                                    l
March 1989 and the documentation closure was completed in
                shared return duct works. The field work was started in             !
September 1993.
                March 1989 and the documentation closure was completed in         !
Post-modification testina was not comoleted.
                September 1993. Post-modification testina was not comoleted.
M12-0-86-006-D provided for the removal of existing HVAC duct work
        .      M12-0-86-006-D provided for the removal of existing HVAC duct work
.
                supports inside the Unit 2 and 3 control room, installed           I
supports inside the Unit 2 and 3 control room, installed
                acoustical tile, installed new duct work including hangers and
acoustical tile, installed new duct work including hangers and
                safety chains. reworked existing ductwork inside the control room,
safety chains. reworked existing ductwork inside the control room,
                and removed existing butterfly dampers inside the control room.
and removed existing butterfly dampers inside the control room.
                The field work was initiated in June 1989 and the work was         l
The field work was initiated in June 1989 and the work was
                determined to be completed in May 1993. Post-modification testina
determined to be completed in May 1993.
                was not completed
Post-modification testina
        .      M12-2/3-82-1 added the HVAC Train B in 1982; however, the NRC's
was not completed
                ISI team concluded the modification was not adeouately tested.     l
M12-2/3-82-1 added the HVAC Train B in 1982; however, the NRC's
        Surveillance Procedure (DTS) 5750-06. Revision 3. " Control Room Standby
.
        HVAC Air Filtration Unit, and Refrigeration Condensing Unit Performance
ISI team concluded the modification was not adeouately tested.
        Requirements." dated August 24, 1996, only required 1/8 iwg positive
Surveillance Procedure (DTS) 5750-06. Revision 3. " Control Room Standby
        pressure in the control room and did not ensure thst pressure was         .
HVAC Air Filtration Unit, and Refrigeration Condensing Unit Performance
        greater than 1/8 iwg for the surrounding areas. In addition, the           l
Requirements." dated August 24, 1996, only required 1/8 iwg positive
        instrumentation used to verify the control room differential
pressure in the control room and did not ensure thst pressure was
        pressure (d)) was not calibrated nor verified to be appro)riate for the
.
        parameters Jeing measured. Specifically, dp Instruments )PI-2-5740-
greater than 1/8 iwg for the surrounding areas.
        31/32 and 36 for the control room and east turbine building had not been
In addition, the
        calibrated. The licensee also identified that the control room
instrumentation used to verify the control room differential
        instrumentation was mislabeled with respect to the areas being sensed
pressure (d)) was not calibrated nor verified to be appro)riate for the
        and, according to '.he drawings, other sensing lines were misrouted or
parameters Jeing measured.
        were broken.
Specifically, dp Instruments )PI-2-5740-
      d. Conclusions
31/32 and 36 for the control room and east turbine building had not been
        The licensee's failure to perform testing of modifications performed to
calibrated. The licensee also identified that the control room
        Unit 2/3 control room HVAC system, as discussed above and detailed in
instrumentation was mislabeled with respect to the areas being sensed
        the ISI Irspection Report 96-201, section 4.6.4.1. dated December 24.
and, according to '.he drawings, other sensing lines were misrouted or
        1996, is an Apparent Violation of 10 CFR 50. Appendix B. Criterion XI.
were broken.
        " Test Controls." (50-237/249-96014-01).
d.
        The apparent violation is being considered for escalated enforcement
Conclusions
        action in accordance with the " General Statement of Policy and Procedure
The licensee's failure to perform testing of modifications performed to
        for NRC Enforcement Actions" (Enforcement Policy). NUREG-1600.
Unit 2/3 control room HVAC system, as discussed above and detailed in
        Accordingly, no Notice of Violation is presently being issued for this
the ISI Irspection Report 96-201, section 4.6.4.1. dated December 24.
        inspection finding. The significance of the issue, and short term
1996, is an Apparent Violation of 10 CFR 50. Appendix B. Criterion XI.
        corrective actions were discussed with the licensee in the exit meeting
" Test Controls." (50-237/249-96014-01).
        for this inspection period on December 19. 1996.
The apparent violation is being considered for escalated enforcement
        Before the NRC makes an enforcement decision, the licensee will be
action in accordance with the " General Statement of Policy and Procedure
        provided an opportucity to respond to the ap)arent violation at a pre-
for NRC Enforcement Actions" (Enforcement Policy). NUREG-1600.
        decisional enforcement conference as descri)ed in the cover letter to
Accordingly, no Notice of Violation is presently being issued for this
        this report.
inspection finding.
                                            13
The significance of the issue, and short term
corrective actions were discussed with the licensee in the exit meeting
for this inspection period on December 19. 1996.
Before the NRC makes an enforcement decision, the licensee will be
provided an opportucity to respond to the ap)arent violation at a pre-
decisional enforcement conference as descri)ed in the cover letter to
this report.
13


  ._     _. _. , _. .             _.__-.._._._.- _ ~ _ _ - . _ . _ _ _ _ . . _ _ _ . . _.                         -
._
      -
_. _. , _. .
  .
_.__-.._._._.- _ ~ _ _ - . _ . _ _ _ _ . . _ _ _ . . _.
                                                                                                                              1
-
                                                                                                                                l
-
          E3        Engineering Procedures and Documentation
.
            E3.1 Additional Vodated Final Safety Analysis Report (UFSAR) Discreoancies
1
                  a. Insoection Scooe (71707)                                                                                 :
E3
                      The inspectors used the UFSAR as a technical reference during a review
Engineering Procedures and Documentation
                      of findings' from a routine drywell tour. A comparison of actual plant
E3.1 Additional Vodated Final Safety Analysis Report (UFSAR) Discreoancies
                      configuration was made to the descriptions contained in the UFSAR. Note
a.
                      that other UFSAR discrepancies regarding the control room HVAC system
Insoection Scooe (71707)
                      were documented in Section E2.1.
:
l                 b. Observations and Findinos                                                                               j
The inspectors used the UFSAR as a technical reference during a review
of findings' from a routine drywell tour. A comparison of actual plant
configuration was made to the descriptions contained in the UFSAR.
Note
that other UFSAR discrepancies regarding the control room HVAC system
were documented in Section E2.1.
l
b.
Observations and Findinos
j
l
!
Prior to performing a Unit 3 drywell routine tour the inspectors
l
l
!                    Prior to performing a Unit 3 drywell routine tour the inspectors
reviewed various UFSAR sections including section 6.1.1.1
l                    reviewed various UFSAR sections including section 6.1.1.1                                   " Materials
" Materials
                      Selection and Fabrication." This section stated, "All piping inside
Selection and Fabrication." This section stated, "All piping inside
'
'
                      containment is covered with metallic mirror-type insulation." During
containment is covered with metallic mirror-type insulation." During
                      the drywell tour the inspectors found this not to be the case as several
the drywell tour the inspectors found this not to be the case as several
i
i
other types of insulation were used on piping. The licensee confirmed
'
'
                      other types of insulation were used on piping. The licensee confirmed
that the other types of insulation ident1fied by the inspectors were
                      that the other types of insulation ident1fied by the inspectors were
acceptable for use in the drywell. This discrepancy was discussed with
                      acceptable for use in the drywell. This discrepancy was discussed with
the licensee and a change to the UFSAR and a performance improvement
                      the licensee and a change to the UFSAR and a performance improvement
form (PIF) were initiated.
                      form (PIF) were initiated.
c.
                  c. Conclusion
Conclusion
                      The above example showed that discrepancies between plant configuration
The above example showed that discrepancies between plant configuration
and the UFSAR still exist.
However, the licensee was taking prompt
!
!
                      and the UFSAR still exist. However, the licensee was taking prompt
actions to resolve identified discrepancies.
                      actions to resolve identified discrepancies.
E4
            E4       Engineering Staff Knowledge and Performance
Engineering Staff Knowledge and Performance
            E4.1 Failure to Uodate Emeraency Diesel Generator (EDG) Vendor Technical
E4.1 Failure to Uodate Emeraency Diesel Generator (EDG) Vendor Technical
                      Information Manual (Units 2 and 3)
Information Manual (Units 2 and 3)
                  a. Insoection Scooe (37551)
a.
                      While inspecting the licensee's response to a Unit 3 EDG test valve
Insoection Scooe (37551)
                      failure (Section 02.2 of this report), the inspectors reviewed the                                       l
While inspecting the licensee's response to a Unit 3 EDG test valve
                      approved vendor technical manual.                                   The inspectors compared the approved
failure (Section 02.2 of this report), the inspectors reviewed the
                      vendor manual to the conditions that existed in the field and conducted-
approved vendor technical manual.
                      discussions with the system engineer and engineering management. The
The inspectors compared the approved
                      following administrative procedures were also reviewed;
vendor manual to the conditions that existed in the field and conducted-
                      e      Dresden Administrative Procedure (DAP) 02-10. " Control of Vendor
discussions with the system engineer and engineering management. The
                              Equipment Technical Information," Revision 5.
following administrative procedures were also reviewed;
                      .      Nuclear Engineering Procedure (NEP) 07-04. "VETIP Process
Dresden Administrative Procedure (DAP) 02-10. " Control of Vendor
,                            Control," Revision 0.
e
Equipment Technical Information," Revision 5.
Nuclear Engineering Procedure (NEP) 07-04. "VETIP Process
.
Control," Revision 0.
,
i
i
                                                                                                                                !
'
                                                                                                                                '
14
                                                                                      14
,
                                                                                                                                l
-
    ,          -                                                               _
_._
_
_ .._
-
.
_.


    -
.
  .
-
      b.  Observations and Findings                                                   l
b.
            The inspectors noted that the test valves depicted in the manual were
Observations and Findings
            different from those installed on the EDGs. During discussion with the       :
The inspectors noted that the test valves depicted in the manual were
            licensee, the correct information was found in the system engineer's
different from those installed on the EDGs.
            desk. Maintaining vendor supplied technical information in an
During discussion with the
            uncontrolled manner was contrary to the licensee's vendor equipment         l
licensee, the correct information was found in the system engineer's
            technical information program (VETIP). Dresden Administrative               !
desk.
            Procedure 02-10. Revision 5. Section E.5 required that " Existing,           i
Maintaining vendor supplied technical information in an
            uncontrolled, and ircoming ETI (Equipment Technical Information) shall
uncontrolled manner was contrary to the licensee's vendor equipment
            be reviewed and added to VETIP so that the latest /most applicable           )
technical information program (VETIP).
            information is available for station use."                                   l
Dresden Administrative
            In addition. NEP 07-04. Section 5.2.1.2. required that "The person
Procedure 02-10. Revision 5. Section E.5 required that " Existing,
            receiving new vendor manual revision data shall forward the information
i
            to the VETIP Coordinator attached to the VETIP Authorization Form
uncontrolled, and ircoming ETI (Equipment Technical Information) shall
            (Exhibit A) or suitable equivalent."
be reviewed and added to VETIP so that the latest /most applicable
            The licensee initiated a PIF documenting the misplaced vendor data and      ;
information is available for station use."
            forwarded the information to the VETIP coordinator for inclusion into        !
            the EDG VETIP manual.                                                        ,
                                                                                        l
      c.  Conclusions                                                                  l
                                                                                        !
            Past weaknesses in the VETIP program were previously documented in
            Inspection Report 96006. section M2.1. dated August 22 1996. The            l
            licensee was not successful in assuring the VETIP was hroperly              i
            implemented. Not entering the EDG test valve technical information          l
            change into the VETIP program as required by approved procedures was a
            Violation of Technical Specification 6.2. Procedures and Programs
            (50-237/249-96014-02).                                                      1
      E4.2 Review of Temocrary Alterations Related to the Control Room HVAC Repair      I
            and the 125Vdc and 250Vdc Batteries (Units 2 and 3)
      a.  Insoection Scooe (37551)
            The inspectors reviewed two installed temporary alterations. The review
            included a field walkdown of the alterations and a review of the
            associated documentation and procedures including:
            .      DAP 05-08. " Control of Temporary System Alterations."
            .      Temporary Alteration No. III-53-96. " Isolate HVAC Supply / Return To
                  and From the Aux Computer Room."
            .      Temporary Alteration No. III-33-96. " Supply Temporary Heat to U2
                  125V and 250V DC Battery Rooms."
      b.  Observations and Findinos
            The auxiliary computer room temporary alteration was installed to
            isolate the room from the control room while the control room walls were
i          sealed. The temporary alteration called for three portable air
l
l
l                                             15
In addition. NEP 07-04. Section 5.2.1.2. required that "The person
receiving new vendor manual revision data shall forward the information
to the VETIP Coordinator attached to the VETIP Authorization Form
(Exhibit A) or suitable equivalent."
The licensee initiated a PIF documenting the misplaced vendor data and
;
forwarded the information to the VETIP coordinator for inclusion into
the EDG VETIP manual.
,
c.
Conclusions
Past weaknesses in the VETIP program were previously documented in
Inspection Report 96006. section M2.1. dated August 22 1996.
The
licensee was not successful in assuring the VETIP was hroperly
implemented.
Not entering the EDG test valve technical information
change into the VETIP program as required by approved procedures was a
Violation of Technical Specification 6.2. Procedures and Programs
(50-237/249-96014-02).
E4.2 Review of Temocrary Alterations Related to the Control Room HVAC Repair
and the 125Vdc and 250Vdc Batteries (Units 2 and 3)
a.
Insoection Scooe (37551)
The inspectors reviewed two installed temporary alterations. The review
included a field walkdown of the alterations and a review of the
associated documentation and procedures including:
DAP 05-08. " Control of Temporary System Alterations."
.
Temporary Alteration No. III-53-96. " Isolate HVAC Supply / Return To
.
and From the Aux Computer Room."
Temporary Alteration No. III-33-96. " Supply Temporary Heat to U2
.
125V and 250V DC Battery Rooms."
b.
Observations and Findinos
The auxiliary computer room temporary alteration was installed to
isolate the room from the control room while the control room walls were
i
sealed.
The temporary alteration called for three portable air
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15


                                          -.
-.
                                                  _ _ . . .__. .
_ _ . .
                                                                      .
.__.
                                                                          _- .   _ . _ _ _ _
.
    -
.
  .
_- .
                                                                                              l
_ . _ _ _ _
                                                                                              :
-
        conditioning (AC) units to be placed in the room and vented out the
.
        auxiliary computer room door. During the walkdown, the inspectors noted
:
        that the door to the room was left open to accommodate the three exhaust
conditioning (AC) units to be placed in the room and vented out the
        trunks used to expel heated exhausts from the portable AC units. This
auxiliary computer room door.
        arrangement essentially countered any benefit received from the AC units
During the walkdown, the inspectors noted
        because of the free exchange of warmer auxiliary electrical room air
that the door to the room was left open to accommodate the three exhaust
;       into the auxiliary computer room.                                                   l
trunks used to expel heated exhausts from the portable AC units.
This
arrangement essentially countered any benefit received from the AC units
because of the free exchange of warmer auxiliary electrical room air
;
into the auxiliary computer room.
l
!
!
        The Unit 2 battery rooms temporary alteration was installed to ensure
The Unit 2 battery rooms temporary alteration was installed to ensure
        that the proper temperature was maintained in the battery rooms while
that the proper temperature was maintained in the battery rooms while
        work was in progress on the normal ventilation system. During the
work was in progress on the normal ventilation system.
        walkdown, the ins)ectors observed that the alteration had been installed
During the
        as intended and tlat a firewatch was present. Both doors to both
walkdown, the ins)ectors observed that the alteration had been installed
        battery rooms were also open which, although allowed by the temporary
as intended and tlat a firewatch was present.
        alteration. seemed unnecessary and even counterproductive to the
Both doors to both
        intended design.
battery rooms were also open which, although allowed by the temporary
        Additionally, the inspectors noted that the battery rooms were about
alteration. seemed unnecessary and even counterproductive to the
        81 F. well abon the required tem)erature of 68 F. This observation was
intended design.
        conveyed to the licensee and the )attery rooms were returned to normal
Additionally, the inspectors noted that the battery rooms were about
        and the firewatch secured. Subsequently, room temperature was monitored
81 F. well abon the required tem)erature of 68 F.
        by hourly operator rounds.
This observation was
        A documentation review showed that the technical evaluation had been
conveyed to the licensee and the )attery rooms were returned to normal
        identified as not safety related. The documented explanation stated
and the firewatch secured.
        that the batteries were safety-related, but the room HVAC system was
Subsequently, room temperature was monitored
        not.
by hourly operator rounds.
        The 125V and 250V batteries were the most risk significant system at the
A documentation review showed that the technical evaluation had been
        facility and were clearly safety-related. The temporary alteration was
identified as not safety related.
        only concerned with maintaining the room temperatures above 68 F to
The documented explanation stated
        assure the batteries were not in a degraded condition. Therefore. the
that the batteries were safety-related, but the room HVAC system was
        installation of the temporary alteration directly affected the two
not.
        station batteries not just the room HVAC.                                           I
The 125V and 250V batteries were the most risk significant system at the
      c. Conclusions
facility and were clearly safety-related. The temporary alteration was
        Although the alterations were installed as written, the design
only concerned with maintaining the room temperatures above 68 F to
        effectiveness was flawed. This appeared to be the result of an
assure the batteries were not in a degraded condition.
        ineffective field walkdown of the alteration and a weak review of the
Therefore. the
        design implementation. Additionally, the licensee maintained that the
installation of the temporary alteration directly affected the two
        battery room alteration only affected the battery room HVAC system and               '
station batteries not just the room HVAC.
        was not safety-related. Further discussions will be needed to resolve
c.
        this issue: therefore this issue will remain an Unresolved Item
Conclusions
          (50-237/249-96014-03).
Although the alterations were installed as written, the design
                                                                                              4
effectiveness was flawed. This appeared to be the result of an
ineffective field walkdown of the alteration and a weak review of the
design implementation.
Additionally, the licensee maintained that the
battery room alteration only affected the battery room HVAC system and
'
was not safety-related.
Further discussions will be needed to resolve
this issue: therefore this issue will remain an Unresolved Item
(50-237/249-96014-03).
4
l
l
l                                           16
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16


  ..   ..     .__ _.   _._______                 ___._-__ _ _                             .       _ __   _
..
    -
..
  .
.__ _.
                                                                                                                j
_._______
                                                                                                                '
___._-__ _ _
.
_
__
_
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-
.
'
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,
E6
Engineering Organization and Administration
l
l
,
,
      E6    Engineering Organization and Administration                                                      l
E6.1 Enaineerina Deoartment Manaaement Chances (37551)
                                                                                                                ,
A new Site Engineering Manager, Mr. Russell Freeman, was ao)ointed
      E6.1 Enaineerina Deoartment Manaaement Chances (37551)
1
,            A new Site Engineering Manager, Mr. Russell Freeman, was ao)ointed                               1
,
l            during the report period. Previously. Mr. Freeman was the )resden Plant                          ;
l            Engineering Superintendent.
      E8    Miscellaneous Engineering Issues (92903)
      E8.1 (Closed) Unresolved Item (50-237/249-95015-05):                  Corner Room Steel.                !
              This issue regarded the corrective action for inadequate corner room                              l
l
l
              structural steel design margins, and was the subject of escalated                                 ;
during the report period.
              enforcement and a civil penalty (EA 96-115) on June 13, 1996. This item                           !
Previously. Mr. Freeman was the )resden Plant
              is closed.                                                                                       !
;
      E8.2 (Closed) Unresolved Item (50-237/249-96013-02): Control Room                                       i
l
Engineering Superintendent.
E8
Miscellaneous Engineering Issues (92903)
E8.1 (Closed) Unresolved Item (50-237/249-95015-05):
Corner Room Steel.
This issue regarded the corrective action for inadequate corner room
l
structural steel design margins, and was the subject of escalated
;
l
enforcement and a civil penalty (EA 96-115) on June 13, 1996.
This item
is closed.
E8.2 (Closed) Unresolved Item (50-237/249-96013-02):
Control Room
i
I
Ventilation System Operability.
This issue regarded the licensee's
'
'
              Ventilation System Operability. This issue regarded the licensee's                                I
corrective actions to resolve inadequate post-modification testing of
              corrective actions to resolve inadequate post-modification testing of
the control room HVAC system. This issue was reviewed and is an example
              the control room HVAC system. This issue was reviewed and is an example
of an apparent violation discussed in Section E2.1 of this re) ort.
              of an apparent violation discussed in Section E2.1 of this re) ort.
Additional followup of this item will be documented against tais reports
              Additional followup of this item will be documented against tais reports                         !
!
assigned tracking number. This item is closed.
,
,
              assigned tracking number. This item is closed.                                                    !
t
                                                                                                                t
IV. Plant Suooort
                                        IV. Plant Suooort
P4
      P4     Staff Knowledge and Performance in EP                                                             '
Staff Knowledge and Performance in EP
      P4.1 Performance durina Assembly Drill (Units 1. 2 and 3)
'
          a. Inspection Scoce (82701)                                                                         ;
P4.1 Performance durina Assembly Drill (Units 1. 2 and 3)
              On November 26 the inspectors observed licensee response to an                                   ,
a.
              unannounced site assembly drill. Documents reviewed included Emergency
Inspection Scoce (82701)
              Plant Im)lementing Procedures (EPIP) 0400-01, " Plant Assembly and                               i
;
              Accounta)ility."
On November 26 the inspectors observed licensee response to an
          b. Observations and Findings
,
              The station alarm was sounded at 1230 and the site assembly drill was
unannounced site assembly drill. Documents reviewed included Emergency
              announced on the station public address system. The inspectors
Plant Im)lementing Procedures (EPIP) 0400-01, " Plant Assembly and
              responded to assigned assembly points and noted that the computerized
i
              assembly card reading system was not operating. After being manually
Accounta)ility."
              accounted, the inspectors went to other assE.3bly areas to observe
b.
              activities.
Observations and Findings
l             In the Administrative Building the accounting 3rocess was in disarray.
The station alarm was sounded at 1230 and the site assembly drill was
              The lunchroom and main hallway were filled wit 1 personnel waiting to be
announced on the station public address system.
              counted.   Twenty minutes into the drill the licensee initiated a manual
The inspectors
l             accounting of personnel in the Administration Building. This was                                 ,
responded to assigned assembly points and noted that the computerized
              accomplished by handing out sheets of paper to management personnel and
assembly card reading system was not operating. After being manually
                                                                                                                '
accounted, the inspectors went to other assE.3bly areas to observe
activities.
l
In the Administrative Building the accounting 3rocess was in disarray.
The lunchroom and main hallway were filled wit 1 personnel waiting to be
counted.
Twenty minutes into the drill the licensee initiated a manual
l
accounting of personnel in the Administration Building.
This was
,
accomplished by handing out sheets of paper to management personnel and
'
'
17
'
'
                                                                                                                '
.
                                                17
. . .
                                    -                       . - . - - - . _ -   -     --     _ _ -     -   _
. -
-
. - . - - -
. _ -
-
--
_ _ -
-
_


  .
.
.
          requiring managers to count assigned personnel. At one point a station
.
          supervisor directed assigned personnel to leave the Administration
requiring managers to count assigned personnel. At one point a station
          Building and go to a work area. This was followed by similar direction
supervisor directed assigned personnel to leave the Administration
          from another su)ervisor. The individual in charge of the accountability
Building and go to a work area. This was followed by similar direction
          activities in t1e Administration Building halted the exodus and stated
from another su)ervisor. The individual in charge of the accountability
          that the accounting for all groups would be completed in the
activities in t1e Administration Building halted the exodus and stated
          Administration Building.
that the accounting for all groups would be completed in the
          The licensee was able to gain control of the accounting process;
Administration Building.
          however, the licensee was not able to complete the accounting within the
The licensee was able to gain control of the accounting process;
          allotted time. Station management determined that aerformance during
however, the licensee was not able to complete the accounting within the
          the drill was unsuccessful and another drill was scleduled. The
allotted time.
          licensee's critique was thorough and independently addressed all of the
Station management determined that aerformance during
          inspectors' concerns.
the drill was unsuccessful and another drill was scleduled.
      c. Conclusions
The
          The difficulty the licensee experienced in accounting for the station
licensee's critique was thorough and independently addressed all of the
          staff manually demonstrated the there had been an over-reliance on the
inspectors' concerns.
          computer counting. The licensee's thorough post-drill critique
c.
          correctiy assessed the weakness in performance and established
Conclusions
          appropriate corrective actions.
The difficulty the licensee experienced in accounting for the station
    F2   Status of Fire Protection Facilities and Equipment
staff manually demonstrated the there had been an over-reliance on the
    F2.1 Problems Identified with Diesel-Driven Fire Pumo (Units 1. 2 and 3)
computer counting. The licensee's thorough post-drill critique
      a. Insoection Scope (64704)
correctiy assessed the weakness in performance and established
          The inspectors performed walkdowns of the Unit 1 diesel-driven fire pump
appropriate corrective actions.
          and all associated equipment and held several discussions with licensee
F2
          staff. The following documentation was also reviewed:
Status of Fire Protection Facilities and Equipment
          .      DAN 901-2 E-8. "U1 Fire PP Day Tank Lvl Hi."
F2.1 Problems Identified with Diesel-Driven Fire Pumo (Units 1. 2 and 3)
          .
a.
                Dresden Fire Protection Surveillance (DFPS) 4123-01. " Unit 1
Insoection Scope (64704)
                Diesel Fire Pump Operability."
The inspectors performed walkdowns of the Unit 1 diesel-driven fire pump
          .      Schematic Diagram 12E-6580F, " Fire Protection System Diesel Driven
and all associated equipment and held several discussions with licensee
                Fire Pump Intake Structure."
staff.
          .      Wiring Diagram 12E-6580G. " Diesel Driven Fire Pump."
The following documentation was also reviewed:
      b. Observations and Findinos
DAN 901-2 E-8. "U1 Fire PP Day Tank Lvl Hi."
          On November 15. the Unit 1 diesel-driven fire pump failed a surveillance
.
          run. The cause for the failure was the closing of the fuel su) ply
Dresden Fire Protection Surveillance (DFPS) 4123-01. " Unit 1
          solenoid valve that occurred when a power lead to the valve vi] rated off
.
          a terminal. During subsequent walkdowns of the pump and associated
Diesel Fire Pump Operability."
          components. the inspectors questioned if the local fuel oil storage tank
Schematic Diagram 12E-6580F, " Fire Protection System Diesel Driven
          level float was operating 3roperly. The work execution center (WEC)
.
          supervisor was contacted a)out the level indicator and stated that the
Fire Pump Intake Structure."
          indicator was working properly. Upon further investigation, the
Wiring Diagram 12E-6580G. " Diesel Driven Fire Pump."
          licensee determined that the level float was not operating properly.
.
                                            18
b.
Observations and Findinos
On November 15. the Unit 1 diesel-driven fire pump failed a surveillance
run. The cause for the failure was the closing of the fuel su) ply
solenoid valve that occurred when a power lead to the valve vi] rated off
a terminal.
During subsequent walkdowns of the pump and associated
components. the inspectors questioned if the local fuel oil storage tank
level float was operating 3roperly. The work execution center (WEC)
supervisor was contacted a)out the level indicator and stated that the
indicator was working properly. Upon further investigation, the
licensee determined that the level float was not operating properly.
18


    -
.
  .
-
            The installed level float indicated the tank was between 3/4 and 7/8
The installed level float indicated the tank was between 3/4 and 7/8
            full, when the tank was only a little more than half full.
full, when the tank was only a little more than half full.
            The inspectors also questioned the low level alarm switch calibrations
The inspectors also questioned the low level alarm switch calibrations
            and requested the latest calibration records. The same WEC supervisor
and requested the latest calibration records. The same WEC supervisor
            was contacted and stated that there was a high level alarm but no low
was contacted and stated that there was a high level alarm but no low
            level alarm on the tank. The inspectors reverified that there was a low
level alarm on the tank.
            level switch, a high and a high-high level switch. The licensee then
The inspectors reverified that there was a low
            determined that the level switches were not in the calibration 3rogram
level switch, a high and a high-high level switch.
            and could not find any documentation of the switches being cali) rated.
The licensee then
            The fuel tank local level indicator float was repaired and the level
determined that the level switches were not in the calibration
            switches were calibrated. The solenoid power lead was reterminated and
3rogram
            the Unit 1 diesel-driven fire pump successfully passed surveillance
and could not find any documentation of the switches being cali) rated.
            testing and was returned to service.                                   '
The fuel tank local level indicator float was repaired and the level
          c. Conclusion
switches were calibrated.
            The fire protection system has had numerous problems over the last few
The solenoid power lead was reterminated and
            months and did not appear to be receiving an adequate level of
the Unit 1 diesel-driven fire pump successfully passed surveillance
            attention. The system operation was not fully understood by some
testing and was returned to service.
            members of the plant staff.
'
      F8   Hiscellaneous Fire Protection Issues (92904)
c.
      F8.1 (Closed) IFT 50-237/249-95008-10: Emergency Lighting. During a fire
Conclusion
i
The fire protection system has had numerous problems over the last few
            protection inspection, the ins)ectors identified that several emergency
months and did not appear to be receiving an adequate level of
            lights were dirty, several lig1ts were aimed improperly, and one light
attention. The system operation was not fully understood by some
            was blocked by a plant modification. The licensee permanently relocated
members of the plant staff.
            the blocked emergency light to a new location. The affected emergency
F8
Hiscellaneous Fire Protection Issues (92904)
F8.1
(Closed) IFT 50-237/249-95008-10:
Emergency Lighting.
During a fire
protection inspection, the ins)ectors identified that several emergency
i
lights were dirty, several lig1ts were aimed improperly, and one light
was blocked by a plant modification. The licensee permanently relocated
the blocked emergency light to a new location. The affected emergency
lights were correctly aimed.
Also, a procedure change was completed to
.
.
'
'
            lights were correctly aimed. Also, a procedure change was completed to
Dresden Electrical Surveillance (DES) 4153-02. Safe Shutdown Emergency
            Dresden Electrical Surveillance (DES) 4153-02. Safe Shutdown Emergency
Lighting Quarterly Inspection, to ensure that emergency lights' lamps
            Lighting Quarterly Inspection, to ensure that emergency lights' lamps
would be inspected and cleaned as necessary.
            would be inspected and cleaned as necessary.   This item is closed.
This item is closed.
                                    VI. Manacement Meetinas
VI. Manacement Meetinas
;     X1   Exit Meeting Summary
;
X1
Exit Meeting Summary
The inspectors 3 resented the inspection results to members of licensee
"
"
            The inspectors 3 resented the inspection results to members of licensee
management at t1e conclusion of the inspection on December 19. 1996.
            management at t1e conclusion of the inspection on December 19. 1996.
The licensee acknowledged the findings presented.
            The licensee acknowledged the findings presented.
The inspectors asked the licensee whether any materials examined during
            The inspectors asked the licensee whether any materials examined during
the inspection should be considered proprietary.
            the inspection should be considered proprietary. No proprietary
No proprietary
            information was identified.
information was identified.
                                                19
19
                                                                                    l
l


                                    . . _ . . _ -
. . _ . . _
    -
-
  .
.
                                                                  ;
-
                                                                  ,
;
,
i
i
                                PARTIAL LIST OF PERSONS CONTACTED !
PARTIAL LIST OF PERSONS CONTACTED
l
!
l
Licensee
!
-
' S. Perry. Vice President. BWR Operations
!
l
E. Connell. Design Engineering Superintendent
;
!
T. Foster. Work Control and Outage Manager
1
R. Freeman. Plant Engineering Superintendent
!
l
J. Heffley. Units 2 and 3 Station Manager
,
C. Howland. Radiation Protection Manager
;
R. Kundalkar. Site Engineering Manager
T. Nauman. Unit 1 Station Manager
l
l
                                                                  !
l      Licensee
                                                                  !
!                                                                -
    ' S. Perry. Vice President. BWR Operations                    !
l      E. Connell. Design Engineering Superintendent              ;
!      T. Foster. Work Control and Outage Manager                1
      R. Freeman. Plant Engineering Superintendent              !
l      J. Heffley. Units 2 and 3 Station Manager                  ,
;      C. Howland. Radiation Protection Manager                    l
      R. Kundalkar. Site Engineering Manager
l
l
      T. Nauman. Unit 1 Station Manager                          l
T. O'Connor. Operations Manager
      T. O'Connor. Operations Manager                             i
i
      F. Spangenburg Regulatory Assurance Manager                 I
F. Spangenburg Regulatory Assurance Manager
I
P. Swafford. Unit 2/3 Maintenance Superintendent
;
;
      P. Swafford. Unit 2/3 Maintenance Superintendent
P. Tzomes. Support Services Director
      P. Tzomes. Support Services Director                       :
:
      D. Winchester. Safety Ouality Verification Director       i
D. Winchester. Safety Ouality Verification Director
                                                                  !
i
                                                                  l
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                                                                  .
                                                                  I
I
I
l                                                                 !
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'
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                                                                  :
                                                          20
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  __ .   -   . .           .   .           . _ ._ _ __.-__ __   _ . . . _ _ . . _ . - _ _ _ . _ . . _ - _ _ _ _ _ . _ _ _ - . _ _
__ .
          -
-
      .
. .
                                                                                                                                    t
.
                                            INSPECTION PROCEDURES USED
.
                                                                                                                                    ,
. _ ._ _ __.-__ __
                IP 37551:   On-site Engineering                                                                                   i
_ . . .
                IP 62707:   Maintenance Observations
_ _ . . _ . - _ _ _ . _ . . _ - _ _ _ _ _ . _ _ _ - . _ _
                IP 64704:   Fire Protection Program
.
                IP 71707:   Plant Operations
-
                IP 82701:   Operational Status of the Emergency Preparedness Program
t
                IP 92901:   Followup - Plant Operations
INSPECTION PROCEDURES USED
                IP 92902:   Followup - Maintenance
,
i                IP 92903:   Followup - Engineering
IP 37551:
l               IP 92904:   Followup - Plant Support
On-site Engineering
i
IP 62707:
Maintenance Observations
IP 64704:
Fire Protection Program
IP 71707:
Plant Operations
IP 82701:
Operational Status of the Emergency Preparedness Program
IP 92901:
Followup - Plant Operations
IP 92902:
Followup - Maintenance
IP 92903:
Followup - Engineering
i
l
IP 92904:
Followup - Plant Support
l
l
                                                                                                                                    !
1
                                                                                                                                    :
                                                                                                                                    1
                                                                                                                                    l
l
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1
1
Line 1,004: Line 1,364:
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21
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Line 1,010: Line 1,370:
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  _ . - _ -           . - - . .__ _ - _ . -         -. . - .
_ . - _ -
              -
. - - .
            .
.__ _ - _ .
                                                                                                  l
-
                                                                                                  l
-. . - .
                                                ITEMS OPENED AND CLOSED
-
l                Ooened                                                                          i
.
i                                                                                                  l
ITEMS OPENED AND CLOSED
l                50-237/249-96014-01 APPARENT Failure to Perform Post-Modification Testing for
l                                            VIO    Control Room HVAC System (Apparent Violation).
l                50-237/249-96014-02      VIO    Failure to Follow VETIP Procedure for Incoming l
                                                    Vendor Technical Information.                  1
                  50-237/249-96014-03      URI    Battery Room Temporary Alteration.
l
l
                  Closed
Ooened
                  50-237:249/95010-03       VIO   Control of Overtime Not Implemented In
i
                                                    Accordance With Generic Letter (GL) 82-12.
i
                  50-237/249-95015-05       URI   Corner Room Steel.
l
                  50-237/249-96013-02       URI   Control Room Ventilation System Operability.
50-237/249-96014-01 APPARENT Failure to Perform Post-Modification Testing for
                  50-237/249-95008-01       IFI   Failure to Follow Procedure Resulted in Two
l
                                                    Inoperable Core Spray Systems.                 !
VIO
                  50-237/249-95008-10       IFI   Emergency Lighting.
Control Room HVAC System (Apparent Violation).
                  50-237:249/96002-04       IFI   Atmospheric Containment Atmosphere Dilution
l
                                                    (ACAD) Operating and Surveillance Procedures'
50-237/249-96014-02
                                                    Bands Differ.
VIO
                                                                                                  l
Failure to Follow VETIP Procedure for Incoming
                                                                                                  l
l
                                                                                                  :
Vendor Technical Information.
                                                                                                  l
1
                                                              22
50-237/249-96014-03
                                                                                                  \
URI
                _ _ _           ,_ .
Battery Room Temporary Alteration.
l
Closed
50-237:249/95010-03
VIO
Control of Overtime Not Implemented In
Accordance With Generic Letter (GL) 82-12.
50-237/249-95015-05
URI
Corner Room Steel.
50-237/249-96013-02
URI
Control Room Ventilation System Operability.
50-237/249-95008-01
IFI
Failure to Follow Procedure Resulted in Two
Inoperable Core Spray Systems.
50-237/249-95008-10
IFI
Emergency Lighting.
50-237:249/96002-04
IFI
Atmospheric Containment Atmosphere Dilution
(ACAD) Operating and Surveillance Procedures'
Bands Differ.
22
_ _ _
,_ .
\\


    ._   _ _ _         . _ . . _   .                 -- _ _. _ _ _ _ . .     .. _ _. _._- . . .
._
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      o
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_ _.
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'
                                                  LIST OF ACRONYM 3 USED
LIST OF ACRONYM 3 USED
                AC             Air Conditioning
AC
i               ACAD           Atmospheric Containment Atmosphere Dilution
Air Conditioning
                ALARA           As Low As Reasonably Achievable                                   I
i
ACAD
Atmospheric Containment Atmosphere Dilution
ALARA
As Low As Reasonably Achievable
CFR
Code of Federal Regulations
4
4
                CFR            Code of Federal Regulations                                      !
.
  .
CRD
                CRD             Coritrol Rod Drive                                                 I
Coritrol Rod Drive
!               DAN             Dresden Annunciator Procedure
!
DAN
Dresden Annunciator Procedure
1
1
                DAP             Dresden Administrative Procedure
DAP
4                DATR           Dresden Administrative Technical Requirements
Dresden Administrative Procedure
                DES             Dresden Electrical Surveillance
DATR
                DFPS           Dresden Fire Protection Surveillance
Dresden Administrative Technical Requirements
                DGP             Dresden General Procedure                                         1
4
DES
Dresden Electrical Surveillance
DFPS
Dresden Fire Protection Surveillance
DGP
Dresden General Procedure
2
2
                DOA             Dresden Operating Abnormal                                         l
DOA
Dresden Operating Abnormal
DOP
Dresden Operating Procedure
;
;
                DOP            Dresden Operating Procedure
DOS
                DOS            Dresden Operations Surveillance
Dresden Operations Surveillance
                dP             Differential Procedure
dP
                DTS             Dresden Technical Surveillance
Differential Procedure
a               EA             Enforcement Action
DTS
;               EDG             Emergency Diesel Generator
Dresden Technical Surveillance
a
EA
Enforcement Action
;
EDG
Emergency Diesel Generator
EPIP
Emergency Plan Implementing Procedures
-
-
                EPIP            Emergency Plan Implementing Procedures
ETI
                ETI            Equipment Technical Information
Equipment Technical Information
;               FME             Foreign Material Exclusion
;
;               GL             Generic Letter
FME
                HPCI           High Pressure Coolant Injection
Foreign Material Exclusion
                HVAC           Heating. Ventilation, and Air Conditioning
;
GL
Generic Letter
HPCI
High Pressure Coolant Injection
HVAC
Heating. Ventilation, and Air Conditioning
HVO
High Voltage Operator
"
"
                HVO            High Voltage Operator
IFI
                IFI            Inspector Followup Item
Inspector Followup Item
                ISI             Independent Safety Inspection
ISI
Independent Safety Inspection
IWG
Inches Water Gage
,
,
'
'
                IWG            Inches Water Gage
LP
                LP              Low Pressure
Low Pressure
;                MG              Motor Generator
                MMD            Mechanical Maintenance Department
:                MWe            Megawatts Electrical
                NEP            Nuclear Engineering Procedure                                    l
J                NDV            Notice of Violation                                                '
l                PDR            Public Document Room                                              j
;                PIF            Performance Improvement Form
                PORC            Plant Operations Review Committee
;                asig          Pounds Per Square Inch Gauge
l                1R              Reactor Recirculation
l                UFSAR          Updated Final Safety Analysis Report
i                URI            Unresolved Item
;
;
                VETIP           Vendor Equipment Technical Information Program
MG
                WEC             Work Execution Center
Motor Generator
MMD
Mechanical Maintenance Department
:
MWe
Megawatts Electrical
NEP
Nuclear Engineering Procedure
J
NDV
Notice of Violation
'
l
PDR
Public Document Room
j
;
PIF
Performance Improvement Form
PORC
Plant Operations Review Committee
asig
Pounds Per Square Inch Gauge
;
l
1R
Reactor Recirculation
l
UFSAR
Updated Final Safety Analysis Report
i
URI
Unresolved Item
;
VETIP
Vendor Equipment Technical Information Program
WEC
Work Execution Center
:
:
i
i
1
1
                                                                          23
23
:I
:I
a
a
}}
}}

Latest revision as of 04:34, 12 December 2024

Insp Repts 50-010/96-14,50-237/96-14 & 50-249/96-14 on 961021-1206.Violations Noted.Major Areas Inspected: Operations,Maintenance,Engineering & Plant Support
ML20134G104
Person / Time
Site: Dresden  Constellation icon.png
Issue date: 02/04/1997
From:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION III)
To:
Shared Package
ML20134G097 List:
References
50-010-96-14, 50-10-96-14, 50-237-96-14, 50-249-96-14, NUDOCS 9702100277
Download: ML20134G104 (23)


See also: IR 05000010/1996014

Text

.

.

U.S. NJCLEAR REGULATORY COMMISSION

REGION III

Docket Nos:

50-10: 50-237: 50-249

License Nos:-

DPR-2: DPR-19: DPR-25

.

Report No:

50-010/96014: 50-237/96014 50-249/96014

Licensee:

Commonwealth Edison Company

Facility:

Dresden Nuclear Station Units 1. 2 and 3

l

Location:

Opus West III

1400 Opus Place - Suite 300

,

l

Downers Grove. IL 60515

,

Dates:

October 21 through December 6. 1996

Inspectors:

C. Vanderniet. Senior Resident Inspector

.

J. Hansen. Resident Inspector

l

D. Roth. Resident Inspector

l

C. Settles. Inspe tor. Illinois Department of

I

Nuclear Sa ety

FAI'

Approved By:

P. L. Hiland. Chief

Reactor Projects Branch 1

9702100277 970204

PDR

ADOCK 05000010

G

PDR

.

.

l

l

i

!

EXECUTIVE SUMMARY

Dresden Nuclear Station Units 1. 2 and 3

iiRC Inspection Report 50-10/96014: 50-237/96014: 50-249/96014

This routine resident inspection included aspects of licensee operations.

maintenance, engineering, and plant support.

The report covered a 7-week

period of resident inspection.

Doerations

The facility was operated in a safe manner and previously identified

.

minor deficiencies were corrected (Section 01.1).

The Unit 3 low pressure heater bay had improved accessibility and

.

housekeeping; however, minor material deficiencies were identified by

the inspectors (Section 01.2).

A manual reactor trip was initiated in response to a loss of the 3B

.

reactor recirculation motor generator set.

Plant and safety equipment

functioned as expected (Section 02.1).

Unit 3 emergency diesel generator (EDG) ejected a cylinder test valve

.

after a surveillance run.

No personnel injuries or significant damage

resulted and after minor repairs the EDG was returned to service

(Section 02.2).

Maintenance

In general, maintenance activities were well controlled: however, two

.

work stoppages were issued due to non-safety related parts control and

contractor work practices (Section M1.1).

l

Significant repair work on the 3B reactor recirculation pump motor was

.

well executed and managed.

Root cause for the motor failure was foreign

material intrusion into the stator windings (Section M2.1).

l

Construction era rag was found inside the Unit 3 high pressure coolant

.

injection (HPCI) lube oil cooler waterbox.

Tube leaks were repaired and

the system was restored to service (Section M2.2).

Enoineerina

The licensee failed to perform post-modification testing on the Unit 2/3

.

main control room heating, ventilation and air conditioning (HVAC)

system. This was an apparent violation (Section E2.1).

An engineer failed to enter vendor technical information into the vendor

.

equipment technical information program (VETIP) as required by plant

procedures (Section E4.1).

2

.

.

Ins)ector review of two tem)orary alterations identified some problems

.

,

wit 1 implementation and tecinical evaluation (Section E4.2).

Plant Support

Computer accounting system failed at the beginning of the plant assembly

.

drill causing confusion. A thorough drill critique identified

deficiencies and corrective actions (Section P4.1).

Problems were identified with the level indication and switch

.

calibration on the Unit 1 diesel-driven fire pump (Section F2.1).

'

1

,

3

-

.

REPORT DETAILS

Summary of Plant Status

Unit 2 began the period at a reduced load of about 300 MWe as some

maintenance activities were concluded. The unit was returned to full

power on October 22.

On October 27 a 2% power derate was initiated due

to feedwater flow instrument uncertainty. On November 23 a load drop

was made to facilitate a drywell entry to add oil to the 2A reactor

recirculation pump motor. The unit was returned to near full power the

following day.

On November 26 the 2% derate was lifted and the unit

returned to full power. On November 28. power was reducea for changing

condensate demineralizes and exercising control rod drives.

The unit

began a slow power increase on December 2 and returned to full power on

December 3.

Unit 3 commenced this inspection period in coastdown in preparation for

refueling outage D3R14. On October 26. the 3B motor generator (MG) set

tripped and after a short period of single loop operations the reactor

was manually tripped on October 27. and a forced outage commenced.

I. OPERATIONS

01

Conduct of Operations

01.1 General Comments (71707)

Routine day-to-day facility operations were observed by inspectors both

in the control room and in the field.

Main control board walkdowns and

reviews of various operating logs were also performed.

Previous

observations discussed in Inspection Re) ort 50-237/249-96013. dated

December 31. 1996 regarding minor breacdowns in control room decorum.

3-way communications, and responsiveness to annunciators were not

observed during this inspection period. Generally, operator performance

inside the control room continued to be crisp and professional. A

weakness was noted with operations personnel outside the control room.

1

specifically, operator knowledge of the Unit 1 diesel-driven fire pump

day tank level switches (paragraph F2.1).

01.2 Tour of Low Pressure Heater Bay (Unit 3)

a.

Insoection Scone (71707)

The inspectors toured Unit 3 low 3ressure heater bay and observed the

general material condition houseceeping, and temporary alterations

installed on heater drain valves.

b.

Observations and Findinos

Overall

the inspectors noted significantly improved housekeeping over

the past nine months; however, numerous undocumented material

discrepancies were identified.

These discrepancies included valves

4

-

.

missing packing gland fasteners. open junction and electrical cable pull

boxes. and misadjusted piping hangers.

After a discussion about general

conditions, several items were identified to the licensee for

correction.

Followup tours of the Unit 3 LP heater bay found that the specific items

had been addressed and a few additional items had been identified by the

licensee.

One of the additional items identified by the licensee was an

o)en lighting junction box above one of the room exits. The tag for

t11s item was attached to a cable tray protective cover through a hole

where the cover bolt and stud had broken off. Additionally. the cover

had several loose or broken nuts, however, none of these deficiencies

were identified by the licensee.

c.

Conclusions

The significant improvement in the housekeeping of the LP heater bay

allowed a greater portion of the room to be more easily accessible.

The

reduction in contaminated areas further improved accessibility to the

room.

However, the identification of material condition problems in

less traveled areas of the plant continued to be a challenge.

02

Operational Status of Facilities and Equipment

02.1 Recirculation Motor-Generator (MG) Set "B" Trio (Unit 3)

a.

Insoection Stone (71707)

On October 26. at 1758 the 3B Recirculation pump tripped due to tri) ping

of the 3B MG set.

Onsite response to this event was performed by t1e

inspectors, and observation of control room personnel performance during

the power reduction and manual reactor scram was accomplished.

The

following operational procedures were reviewed:

Dresden Annunciator Procedure (DAN) 903-4 A6. 3B RECIRC M-G SET

.

GEN LOCKOUT.

DAN 903-4 A7. 3B RECIRC PP DP LO.

.

DAN 903-4 08, 3B RECIRC PP LOWER LUBE OIL LVL LO.

.

Dresden Operating Abnormal (DOA) 0202-01. Recirculation Pump Trip

.

One or Both Pumps.

Dresden General Procedure (DGP) 02-01. Unit 2 (3) NORMAL UNIT

.

SHUTDOWN

DGP 02-03. REACTOR SCRAM

.

DGP 03-03. SINGLE RECIRCULATION LOOP OPERATION

.

b.

Observations and Findinos

l

l

The root cause of the MG set trip was not immediately known and single

loop operation commenced.

The inspectors responded to the site and

l

i

monitored the reactor down power and the subsequent manual reactor trip

at 0201 on October 27. After the 3B MG set tripped, the 3A MG set was

reduced to 60 percent power in accordance with approved procedures and

5

l

l

i

!

l

.

.

the unit was stabilized at about 34 percent power.

Power was further

decreased to 25 percent using recirculation flow and a manual reactor trip signal initiated.

Systems responded as expected with the exception

of rod position indication failures for two rods and two intermediate

range monitor failures.

For the evolutions observed plant operators

followed all appropriate procedures during the course of the shutdown.

Control room decorum and 3-way communications were maintained throughout

the event.

c.

Conclusion

The plant response to the loss of a single reactor recirculation pump

was in accordance with expectations and plant design.

The control room

operators followed procedures and conducted an orderly shutdown.

02.2 Emergency Diesel Generator (EDG) E.iected a Cylinder Test Valve Durina

Troubleshootina Run (Unit 3)

a.

Inspection Scone (71707)

The inspectors observed a test of the Unit 3 EDG and observed the

licensee's response to the observed test failure.

Field observations,

system and equipment inspection walkdowns were performed before and

after the valve ejection occurred.

Additionally, the inspectors

reviewed the following documentation

Vendor Equipment Technical Information Program (VETIP) Manual

.

1163. Electro-Motive Diesel Engine.

Dresden Electrical Surveillance (DTS) 6600-01. Diesel Generator

.

Governor Oil Change and Compensation Adjustment

Dresden Operations Surveillance (DOS) 6600-01. " Diesel Generator

.

Surveillance Test."

b.

Observations and Findinas

On November 24. the inspectors observed performance of Dresden

Electrical Surveillance (DTS) 6600-01 for the Unit 3 EDG.

No

abnormalities were noted during the initial performance of the test.

Subsequent to test performance, the Shift Manager informed the

inspectors that the EDG had ejected a cylinder test valve from

Cylinder 20.

The High Voltage Operator (HVO) had entered the room to

secure the EDG and reported that the test valve had blown out.

The

inspectors returned to the Unit 3 EDG room shortly after the EDG was

secured.

I

The test valve had blown out of Cylinder 20 on the EDG generator end.

The valve appeared to have impacted the wall directly adjacent to the

valve and fallen to the floor.

No damage was evident from the valve

ejection, other than carbon buildup on piping near the cylinder test

valve port.

Inspection of the test valve showed no damage or unusual

wear.

No personnel injuries were reported and the licensee immediately

i

initiated a prompt investigation into the event.

)

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During additional inspection on November 25. the inspectors noted that

.

the Unit 3 EDG cylinder test valves did not appear to be threaded into

1

the cylinder block as far as the test valves on the Unit 2 or 2/3 EDGs.

l

1

This information was conveyed to the licensee's team performing the

!

prompt event investigation.

l

The prompt investigation c termined that the test valves had been

j

replaced in December 1995, and that the ejected valve must have had a

,

relaxed torque that was further loosened due to normal EDG vibrations.

'

Additionally. Cylinder 20 on the Unit 3 EDG was the cylinder with the

highest compression pressure on the engine. The licensee did not

perform a formal root cause evaluation of this event although several

corrective actions were performed.

The EDG was repaired and was

i

returned to service on November 27.

c.

Conclusions

Operations personnel performed the surveillance testing in accordance

with the appropriate procedures and were observed closely monitoring EDG

performance.

08

Miscellaneous Operations Issues (92700)

08.1

(Closed) Violation (50-237:249/95010-03):

Control of Overtime Not

Implemented In Accordance With Generic Letter (GL) 82-12.

Revision 1 to

Dresden Operating Procedure 01-09. Control of Overtime authorized

November 14, 1995, incorporated the guidance established in GL 82-12.

This action appeared adequate to prevent recurrence: however, the

recently completed independent safety inspection (ref. IR 50-237:249/96-

201, dated December 24, 1996. Section 6.3.3) identified continuing

problems with corrective action for control of overtime. This item is

closed and further followup will be documented against Independent

Safety Inspection (ISI) Deficiency 50-237:249/96-201-29

08.2 (Closed) Insoector Followuo item (IFI) 50-237:249/96002-04:

Atmospheric

Containment Atmosphere Dilution (ACAD) Operating and Surveillance

Procedures' Bands Differ. The inspectors noted that the ACAD system air

receiver operating pressure band was being maintained at 44 to 57 psig,

which was above the band in Dresden Operating Procedure (DOP) 2500-01.

"ACAD Dilution Subsystem Operation" (41 to 52 psig).

Dresden Operating

Surveillance (DOS) 2500-01. "ACAD Compressor Surveillance," and Dresden

Administrative Technical Requirements (DATR) both listed a pressure band

of 44 to 57 psig.

To resolve this issue, the licensee planned to revise

the appropriate ACAD procedures.

The inspector reviewed the revised

ACAD procedure (DOP 2500-01) and the changes to the UFSAR and had no

further concerns. This item is closed.

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II. Maintenance

'

M1

Conduct of Haintenance

l

M1.1 General Comments (62707)

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In general, maintenance activities at the facility were well controlled

and performed in accordance with approved work packages and procedures.

Numerous tasks were observed in the field and minor observations were

discussed with the appropriate licensee staff.

Scheduling and work

planning continued to be difficult 3roblems.

This was evident when a

stop work order was issued during t1e conduct of maintenance which left

an oil pump for both the 2A and 2B MG set oil skids out of service,

thereby leaving both MG sets in a more vulnerable condition.

Significant work activities that were performed during this inspection

.

period not receiving specific comment included the following;

3D Electromatic Relief Valve Flange Leak Repair

.

Unit 3 EDG Power Pack Replacement

.

Additionally, during this report period the licensee issued two stop

work orders. The first, issued November 21. regarded the retraining of

contractor personnel in the use of nuclear standard work procedures.

i

This was in response to a failure of contract worker personnel to comply

with facility safe work practices. The second, issued November 24

regarded the procurement and use of non-safety related parts.

This was

partially in response to the 3A control rod drive pump discharge

isolation valve that was installed with a through wall pinhole leak.

Both work stoppages were of short duration and were appropriate

resomses to address specific maintenance problems.

H2

Maintenance Material Condition of Facility and Equipment

M2.1

"B" Reactor Recirculation (RR) Pumo Motor Repair (Unit 3)

a.

Inspection Scope (62707)

During the report period, the inspectors observed licensee actions to

troubleshoot and repair the 3B reactor recirculation (RR) motor trip.

Portions of the field preparation and actual repair were observed by the

inspectors.

In addition, work package preparation and s3ecial rigging

and load testing documentation were reviewed including t1e following:

Vendor Manual GEK-26132. " Boiling Water Nuclear Reactor

.

Recirculating Water Pump Motors for the Dresden 11 and III nuclear

power station of the Commonwealth Edison Company by the General

Electric Atomic Power Equipment Department."

Special Procedure (SP) 96-11-019. "3B RR Pump Motor In-place

.

Repair."

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Dresden Engineering Document 5254777. " Reactor Recirculation Pump

Motor Refurbishment - Details for the Engineered Impact Mat -

Unit 3."

Dresden Engineering Document 5257492. " Reactor Recirculation Pump

.

Motor Refurbishment - Details for Pump Bowl Shimming. Engineered

Impact Mat and Rigging."

Dresden Engineering Document 5253222. " Rigging of the 3B Recir.

.

Pump Motor End Bell. Rotor and Stator to Repair the Motor in

Place."

b.

Observations and Findinas

After the October 26, 3B RR pump MG set trip. the licensee's

,

troubleshooting effort located a ground in the pump motor. Two

approaches to resolve the problem were developed; repair the motor in-

'

place, or replacement with a rebuilt motor. A rebuilt motor was

obtained and brought to the site, but work to repair in-place continued.

The repair work included load-testing the drywell monorail: design.

testing, and installation of an engineered impact mat: development of a

rigging plan for the motor endbell, rotor and stator; and identifying

j

possible repair techniques. The plan called for the removal of the

motor endbell and rotor and the lifting of the stator.

The stator

needed to be lifted high enough to allow access for inspection and

repair.

Once the package was finally prepared, a special )lant

operations review committee (PORC) reviewed and approved t1e plan.

During the preparation of the work, the inspectors reviewed selected

portions of the packages and observed monorail and impact mat testing.

j

The use of a computer-generated animation of the lifting process greatly

aided all personnel in understanding the job. Also, the assignment of

the Operations Manager as a dedicated project manager ensured continuity

on the project.

During the stator inspection a small piece of banding material was

discovered shorting one motor phase. The foreign material was removed

and the damaged area of the windings repaired. After successfully

testing the windings, the motor was reassembled.

The piece of banding

,

material most likely entered the motor in late 1990 to early 1991 time

frame when the endbell had been removed for maintenance. The banding

material was similar to material used to secure component identification

label plates inside the drywell. The licensee suspected that some of

this material was dropped into the motor and eventually shorted the

stator.

Additional foreign material found inside the motor was removed.

The intrusion of foreign material into various components at the

facility has been a longstanding problem.

However, the inspectors'

recent observations of foreign material exclusion (ME) practices

indicated that significant improvements have been made over past

practices.

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The ins)ectors observed various activities as the work progressed and

noted tlat the job was well managed and skillfully performed.

Disassembly, re) air. and reassembly progressed as expected and no major

problems with t1e work plans were encountered.

Radiation protection

controls and practices were followed and the use of a video monitor for

the viewing of the work was a good "as low as reasonably achievable"

t

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(ALARA) practice.

c.

Conclusions

The 3B RR pump motor repair was well coordinated.

Management and Site

Quality Verification oversight were maintained and no significant

!

unanticipated problems occurred. The finding of several pieces of

foreign material inside a major component was not a new issue at the

facility and efforts to improve FME continued to receive appropriate

management attention.

M2.2 Rao Found in Hiah Pressure Coolant Iniection (HPCI) Lube Oil Cooler.

(Unit 2)

a.

Inspection Scone (62707)

The inspectors ins)ected the Unit 2 HPCI lube oil cooler and observed

the rag found by t1e licensee during emergent maintenance work. A

review of the licensee's efforts to identify when the rag entered the

system was also performed,

b.

Observations and Findinas

The HPCI system was declared inoperable on November 27. due to excessive

l

water contamination in the turbine lubricating oil.

While performing

i

maintenance to repair the water leaks in the lube oil cooler,

maintenance personnel discovered a rag in the cooler water box. The rag

covered a significant portion of the cooler tube openings and appeared

to have been acting as a filter for the cooling medium.

The licensee suspects that the rag had been used as an FME cover during

facility construction and was never removed.

The assumption was

substantiated due to the lack of finding any previous maintenance items

that required removal of the HPCI lube oil cooler endbells in the

maintenance database.

Further database searches showed that no recorded

maintenance work had been performed on the cooler or cooling system that

would have allowed visual identification of the rag since the system was

originally placed in service. The licensee also reviewed surveillance

test data and did not identify any instance of the HPCI system being

inoperable or degraded due to inadequate lube oil cooler performance.

Repair efforts were completed and the cooler was reassembled and

satisfactorily tested.

Unit 2 HPCI was returned to service on

December 1, with no further problems.

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c.

Conclusions

i-

All observed maintenance activities were performed in a skilled manner,

i

however, the discovery of the rag in the cooler further emphasized the

i

need to continue monitoring FME controls.

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Miscellaneous Maintenance Issues (92902)

M8

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M8.1

(Closed) Insoector Followuo Item 50-237/249-95008-01:

Failure to Follow

Procedure Resulted in Two Inoperable Core Spray Systems.

On April 24,

'

1995, the licensee reused o-rings on environmentally qualified equipment

}

and only hand tightened the transmitter covers in violation of the

3rocedure. The inspectors reviewed information on reused o-rings and

)

.

land tightened covers in CHRON # 0308805 and a referenced letter from

'

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Rosemount.

The information a)peared adequate to support the licensee's

l

operability determination. T11s item is closed.

a

III. Enaineerina

E2

Engineering Support of Facilities and Equipment

E2.1 Failure to Perform Adeouate Post-Modification Testina of the Control

Room Heatina and Air Conditionina (HVAC) System (Units 1. 2 and 3)

a.

Insoection Scope (37551)

The inspectors continued to observe and monitor the licensee's progress

in correcting control room HVAC design and testing deficiencies.

The

following documentation was reviewed:

Modifications M12-2/3-82-1. M12-0-87-005 and M12-0-86-006:

Unit 1

.

Control Room Modifications.

DTS 5750-06, " Control Room Standby HVAC Air Filtration Unit, and

Refrigeration Condensing Unit Performance Requirements," dated

August 24, 1996.

b.

Observations and Findinas

The licensee continued work on sealing penetrations into the Unit 2/3

control room, auxiliary computer room, and train "B" HVAC rcom.

At the

close of this report period, efforts to remove a temporary alteration

and return the auxiliary computer roo.n into the control room envelope

were unsuccessful.

The licensee continued testing and achieved and

maintained positive pressure requirements with the exception of the

auxiliary computer room.

Further work was planned to correct problems

in the computer room and return the room to the control room envelope.

Background information on this issue can be found in Inspection Report

96013 (paragraph E2.4) and Independent Safety Inspection (ISI) Report

96-201 (paragraph 4.6.4.1).

The significance of this event was

previously considered an Unresolved Item (50-237:249/95013-02).

11

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c.

ISI Report 96-201. dated December 24. 1997. Daragraoh 4.6.4.1

Sections 6.4.2 and 9.4-3 of the UFSAR described the design basis for the

control room HVAC system.

Section 6.4.2.4 stated that potential adverse

interactions between the control room emergency zone and adjacent zones

that may allow the transfer of toxic or radioactive gases into the

control room were minimized by maintaining the control room at a

positive pressure of 1/8-inch water gauge (iwg) during emergency

,

pressurization modes, and with respect to adjacent areas.

On October 8. 1996, the licensee declared the control room HVAC system

inoperable because of the inability to maintain the control room at a

positive pressure during normal operations and at 1/8 iwg with respect

to the surrounding areas in the emergency mode.

The control room

ventilation system had not been maintained or properly tested 'o ensure

that the system operated within its design basis.

Modifications had

been implemented, or partially implemented, which resulted in negative

l

pressure within the control room and the inability to pressurize the

control room to 1/8 iwg in the emergency mode.

In addition,

instrumentation that was used to verify the control room pressure was

positive in the emergency mode had not been calibrated, and had not been

installed in accordance with the piping and instrumentation diagram.

j

i

In September 1996, the licensee began reviewirg open modifications for

'

the control room ventilation system, and subsequently determined that

several control room modifications, which had not been completed,

i

contributed to the inability to pressurize the control room as stated in

the UFSAR.

These incomplete modifications were identified as a result

,

of the licensee's efforts to close all modifications or approve the as-

I

built configuration.

The specific modifications affecting the control

room included:

M12-0-87-005-D provided for the installation of security equipment

.

such as bullet resistant plating for walls and ceilings, new east-

3

west kitchen and locker room area fire and non-fire rated doors.

I

and the sealing of new and unused wall and floor penetrations.

Field work was initiated in August 1991 and completed in

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January 1992.

Post-modification testina was not oerformed.

l

M12-0-87-005-E provided supply and exhaust ventilation systems for

i

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the new locker room and kitchen areas, new fire dampers in duct

work penetrating fire walls, control logic for operation of the

isolation dampers, and an interlock for the exhaust fans from the

isolation dampers.

Field work was started in September 1991 and

l

completed by June 1993. The oost-modification testina, includina

loaic testina and emergency oressurization testina to verify

1/8 iwa was not oerformed.

M12-0-86-006-C provided supply and return side duct silencers,

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thermally insulated duct work, and manual volume dampers in the

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shared return duct works.

The field work was started in

March 1989 and the documentation closure was completed in

September 1993.

Post-modification testina was not comoleted.

M12-0-86-006-D provided for the removal of existing HVAC duct work

.

supports inside the Unit 2 and 3 control room, installed

acoustical tile, installed new duct work including hangers and

safety chains. reworked existing ductwork inside the control room,

and removed existing butterfly dampers inside the control room.

The field work was initiated in June 1989 and the work was

determined to be completed in May 1993.

Post-modification testina

was not completed

M12-2/3-82-1 added the HVAC Train B in 1982; however, the NRC's

.

ISI team concluded the modification was not adeouately tested.

Surveillance Procedure (DTS) 5750-06. Revision 3. " Control Room Standby

HVAC Air Filtration Unit, and Refrigeration Condensing Unit Performance

Requirements." dated August 24, 1996, only required 1/8 iwg positive

pressure in the control room and did not ensure thst pressure was

.

greater than 1/8 iwg for the surrounding areas.

In addition, the

instrumentation used to verify the control room differential

pressure (d)) was not calibrated nor verified to be appro)riate for the

parameters Jeing measured.

Specifically, dp Instruments )PI-2-5740-

31/32 and 36 for the control room and east turbine building had not been

calibrated. The licensee also identified that the control room

instrumentation was mislabeled with respect to the areas being sensed

and, according to '.he drawings, other sensing lines were misrouted or

were broken.

d.

Conclusions

The licensee's failure to perform testing of modifications performed to

Unit 2/3 control room HVAC system, as discussed above and detailed in

the ISI Irspection Report 96-201, section 4.6.4.1. dated December 24.

1996, is an Apparent Violation of 10 CFR 50. Appendix B. Criterion XI.

" Test Controls." (50-237/249-96014-01).

The apparent violation is being considered for escalated enforcement

action in accordance with the " General Statement of Policy and Procedure

for NRC Enforcement Actions" (Enforcement Policy). NUREG-1600.

Accordingly, no Notice of Violation is presently being issued for this

inspection finding.

The significance of the issue, and short term

corrective actions were discussed with the licensee in the exit meeting

for this inspection period on December 19. 1996.

Before the NRC makes an enforcement decision, the licensee will be

provided an opportucity to respond to the ap)arent violation at a pre-

decisional enforcement conference as descri)ed in the cover letter to

this report.

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E3

Engineering Procedures and Documentation

E3.1 Additional Vodated Final Safety Analysis Report (UFSAR) Discreoancies

a.

Insoection Scooe (71707)

The inspectors used the UFSAR as a technical reference during a review

of findings' from a routine drywell tour. A comparison of actual plant

configuration was made to the descriptions contained in the UFSAR.

Note

that other UFSAR discrepancies regarding the control room HVAC system

were documented in Section E2.1.

l

b.

Observations and Findinos

j

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Prior to performing a Unit 3 drywell routine tour the inspectors

l

reviewed various UFSAR sections including section 6.1.1.1

" Materials

Selection and Fabrication." This section stated, "All piping inside

'

containment is covered with metallic mirror-type insulation." During

the drywell tour the inspectors found this not to be the case as several

i

other types of insulation were used on piping. The licensee confirmed

'

that the other types of insulation ident1fied by the inspectors were

acceptable for use in the drywell. This discrepancy was discussed with

the licensee and a change to the UFSAR and a performance improvement

form (PIF) were initiated.

c.

Conclusion

The above example showed that discrepancies between plant configuration

and the UFSAR still exist.

However, the licensee was taking prompt

!

actions to resolve identified discrepancies.

E4

Engineering Staff Knowledge and Performance

E4.1 Failure to Uodate Emeraency Diesel Generator (EDG) Vendor Technical

Information Manual (Units 2 and 3)

a.

Insoection Scooe (37551)

While inspecting the licensee's response to a Unit 3 EDG test valve

failure (Section 02.2 of this report), the inspectors reviewed the

approved vendor technical manual.

The inspectors compared the approved

vendor manual to the conditions that existed in the field and conducted-

discussions with the system engineer and engineering management. The

following administrative procedures were also reviewed;

Dresden Administrative Procedure (DAP) 02-10. " Control of Vendor

e

Equipment Technical Information," Revision 5.

Nuclear Engineering Procedure (NEP) 07-04. "VETIP Process

.

Control," Revision 0.

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b.

Observations and Findings

The inspectors noted that the test valves depicted in the manual were

different from those installed on the EDGs.

During discussion with the

licensee, the correct information was found in the system engineer's

desk.

Maintaining vendor supplied technical information in an

uncontrolled manner was contrary to the licensee's vendor equipment

technical information program (VETIP).

Dresden Administrative

Procedure 02-10. Revision 5. Section E.5 required that " Existing,

i

uncontrolled, and ircoming ETI (Equipment Technical Information) shall

be reviewed and added to VETIP so that the latest /most applicable

information is available for station use."

l

In addition. NEP 07-04. Section 5.2.1.2. required that "The person

receiving new vendor manual revision data shall forward the information

to the VETIP Coordinator attached to the VETIP Authorization Form

(Exhibit A) or suitable equivalent."

The licensee initiated a PIF documenting the misplaced vendor data and

forwarded the information to the VETIP coordinator for inclusion into

the EDG VETIP manual.

,

c.

Conclusions

Past weaknesses in the VETIP program were previously documented in

Inspection Report 96006. section M2.1. dated August 22 1996.

The

licensee was not successful in assuring the VETIP was hroperly

implemented.

Not entering the EDG test valve technical information

change into the VETIP program as required by approved procedures was a

Violation of Technical Specification 6.2. Procedures and Programs

(50-237/249-96014-02).

E4.2 Review of Temocrary Alterations Related to the Control Room HVAC Repair

and the 125Vdc and 250Vdc Batteries (Units 2 and 3)

a.

Insoection Scooe (37551)

The inspectors reviewed two installed temporary alterations. The review

included a field walkdown of the alterations and a review of the

associated documentation and procedures including:

DAP 05-08. " Control of Temporary System Alterations."

.

Temporary Alteration No. III-53-96. " Isolate HVAC Supply / Return To

.

and From the Aux Computer Room."

Temporary Alteration No. III-33-96. " Supply Temporary Heat to U2

.

125V and 250V DC Battery Rooms."

b.

Observations and Findinos

The auxiliary computer room temporary alteration was installed to

isolate the room from the control room while the control room walls were

i

sealed.

The temporary alteration called for three portable air

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conditioning (AC) units to be placed in the room and vented out the

auxiliary computer room door.

During the walkdown, the inspectors noted

that the door to the room was left open to accommodate the three exhaust

trunks used to expel heated exhausts from the portable AC units.

This

arrangement essentially countered any benefit received from the AC units

because of the free exchange of warmer auxiliary electrical room air

into the auxiliary computer room.

l

!

The Unit 2 battery rooms temporary alteration was installed to ensure

that the proper temperature was maintained in the battery rooms while

work was in progress on the normal ventilation system.

During the

walkdown, the ins)ectors observed that the alteration had been installed

as intended and tlat a firewatch was present.

Both doors to both

battery rooms were also open which, although allowed by the temporary

alteration. seemed unnecessary and even counterproductive to the

intended design.

Additionally, the inspectors noted that the battery rooms were about

81 F. well abon the required tem)erature of 68 F.

This observation was

conveyed to the licensee and the )attery rooms were returned to normal

and the firewatch secured.

Subsequently, room temperature was monitored

by hourly operator rounds.

A documentation review showed that the technical evaluation had been

identified as not safety related.

The documented explanation stated

that the batteries were safety-related, but the room HVAC system was

not.

The 125V and 250V batteries were the most risk significant system at the

facility and were clearly safety-related. The temporary alteration was

only concerned with maintaining the room temperatures above 68 F to

assure the batteries were not in a degraded condition.

Therefore. the

installation of the temporary alteration directly affected the two

station batteries not just the room HVAC.

c.

Conclusions

Although the alterations were installed as written, the design

effectiveness was flawed. This appeared to be the result of an

ineffective field walkdown of the alteration and a weak review of the

design implementation.

Additionally, the licensee maintained that the

battery room alteration only affected the battery room HVAC system and

'

was not safety-related.

Further discussions will be needed to resolve

this issue: therefore this issue will remain an Unresolved Item

(50-237/249-96014-03).

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E6

Engineering Organization and Administration

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E6.1 Enaineerina Deoartment Manaaement Chances (37551)

A new Site Engineering Manager, Mr. Russell Freeman, was ao)ointed

1

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during the report period.

Previously. Mr. Freeman was the )resden Plant

l

Engineering Superintendent.

E8

Miscellaneous Engineering Issues (92903)

E8.1 (Closed) Unresolved Item (50-237/249-95015-05):

Corner Room Steel.

This issue regarded the corrective action for inadequate corner room

l

structural steel design margins, and was the subject of escalated

l

enforcement and a civil penalty (EA 96-115) on June 13, 1996.

This item

is closed.

E8.2 (Closed) Unresolved Item (50-237/249-96013-02):

Control Room

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Ventilation System Operability.

This issue regarded the licensee's

'

corrective actions to resolve inadequate post-modification testing of

the control room HVAC system. This issue was reviewed and is an example

of an apparent violation discussed in Section E2.1 of this re) ort.

Additional followup of this item will be documented against tais reports

!

assigned tracking number. This item is closed.

,

t

IV. Plant Suooort

P4

Staff Knowledge and Performance in EP

'

P4.1 Performance durina Assembly Drill (Units 1. 2 and 3)

a.

Inspection Scoce (82701)

On November 26 the inspectors observed licensee response to an

,

unannounced site assembly drill. Documents reviewed included Emergency

Plant Im)lementing Procedures (EPIP) 0400-01, " Plant Assembly and

i

Accounta)ility."

b.

Observations and Findings

The station alarm was sounded at 1230 and the site assembly drill was

announced on the station public address system.

The inspectors

responded to assigned assembly points and noted that the computerized

assembly card reading system was not operating. After being manually

accounted, the inspectors went to other assE.3bly areas to observe

activities.

l

In the Administrative Building the accounting 3rocess was in disarray.

The lunchroom and main hallway were filled wit 1 personnel waiting to be

counted.

Twenty minutes into the drill the licensee initiated a manual

l

accounting of personnel in the Administration Building.

This was

,

accomplished by handing out sheets of paper to management personnel and

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requiring managers to count assigned personnel. At one point a station

supervisor directed assigned personnel to leave the Administration

Building and go to a work area. This was followed by similar direction

from another su)ervisor. The individual in charge of the accountability

activities in t1e Administration Building halted the exodus and stated

that the accounting for all groups would be completed in the

Administration Building.

The licensee was able to gain control of the accounting process;

however, the licensee was not able to complete the accounting within the

allotted time.

Station management determined that aerformance during

the drill was unsuccessful and another drill was scleduled.

The

licensee's critique was thorough and independently addressed all of the

inspectors' concerns.

c.

Conclusions

The difficulty the licensee experienced in accounting for the station

staff manually demonstrated the there had been an over-reliance on the

computer counting. The licensee's thorough post-drill critique

correctiy assessed the weakness in performance and established

appropriate corrective actions.

F2

Status of Fire Protection Facilities and Equipment

F2.1 Problems Identified with Diesel-Driven Fire Pumo (Units 1. 2 and 3)

a.

Insoection Scope (64704)

The inspectors performed walkdowns of the Unit 1 diesel-driven fire pump

and all associated equipment and held several discussions with licensee

staff.

The following documentation was also reviewed:

DAN 901-2 E-8. "U1 Fire PP Day Tank Lvl Hi."

.

Dresden Fire Protection Surveillance (DFPS) 4123-01. " Unit 1

.

Diesel Fire Pump Operability."

Schematic Diagram 12E-6580F, " Fire Protection System Diesel Driven

.

Fire Pump Intake Structure."

Wiring Diagram 12E-6580G. " Diesel Driven Fire Pump."

.

b.

Observations and Findinos

On November 15. the Unit 1 diesel-driven fire pump failed a surveillance

run. The cause for the failure was the closing of the fuel su) ply

solenoid valve that occurred when a power lead to the valve vi] rated off

a terminal.

During subsequent walkdowns of the pump and associated

components. the inspectors questioned if the local fuel oil storage tank

level float was operating 3roperly. The work execution center (WEC)

supervisor was contacted a)out the level indicator and stated that the

indicator was working properly. Upon further investigation, the

licensee determined that the level float was not operating properly.

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The installed level float indicated the tank was between 3/4 and 7/8

full, when the tank was only a little more than half full.

The inspectors also questioned the low level alarm switch calibrations

and requested the latest calibration records. The same WEC supervisor

was contacted and stated that there was a high level alarm but no low

level alarm on the tank.

The inspectors reverified that there was a low

level switch, a high and a high-high level switch.

The licensee then

determined that the level switches were not in the calibration

3rogram

and could not find any documentation of the switches being cali) rated.

The fuel tank local level indicator float was repaired and the level

switches were calibrated.

The solenoid power lead was reterminated and

the Unit 1 diesel-driven fire pump successfully passed surveillance

testing and was returned to service.

'

c.

Conclusion

The fire protection system has had numerous problems over the last few

months and did not appear to be receiving an adequate level of

attention. The system operation was not fully understood by some

members of the plant staff.

F8

Hiscellaneous Fire Protection Issues (92904)

F8.1

(Closed) IFT 50-237/249-95008-10:

Emergency Lighting.

During a fire

protection inspection, the ins)ectors identified that several emergency

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lights were dirty, several lig1ts were aimed improperly, and one light

was blocked by a plant modification. The licensee permanently relocated

the blocked emergency light to a new location. The affected emergency

lights were correctly aimed.

Also, a procedure change was completed to

.

'

Dresden Electrical Surveillance (DES) 4153-02. Safe Shutdown Emergency

Lighting Quarterly Inspection, to ensure that emergency lights' lamps

would be inspected and cleaned as necessary.

This item is closed.

VI. Manacement Meetinas

X1

Exit Meeting Summary

The inspectors 3 resented the inspection results to members of licensee

"

management at t1e conclusion of the inspection on December 19. 1996.

The licensee acknowledged the findings presented.

The inspectors asked the licensee whether any materials examined during

the inspection should be considered proprietary.

No proprietary

information was identified.

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PARTIAL LIST OF PERSONS CONTACTED

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Licensee

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' S. Perry. Vice President. BWR Operations

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E. Connell. Design Engineering Superintendent

!

T. Foster. Work Control and Outage Manager

1

R. Freeman. Plant Engineering Superintendent

!

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J. Heffley. Units 2 and 3 Station Manager

,

C. Howland. Radiation Protection Manager

R. Kundalkar. Site Engineering Manager

T. Nauman. Unit 1 Station Manager

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T. O'Connor. Operations Manager

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F. Spangenburg Regulatory Assurance Manager

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P. Swafford. Unit 2/3 Maintenance Superintendent

P. Tzomes. Support Services Director

D. Winchester. Safety Ouality Verification Director

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INSPECTION PROCEDURES USED

,

IP 37551:

On-site Engineering

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IP 62707:

Maintenance Observations

IP 64704:

Fire Protection Program

IP 71707:

Plant Operations

IP 82701:

Operational Status of the Emergency Preparedness Program

IP 92901:

Followup - Plant Operations

IP 92902:

Followup - Maintenance

IP 92903:

Followup - Engineering

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IP 92904:

Followup - Plant Support

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ITEMS OPENED AND CLOSED

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Ooened

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50-237/249-96014-01 APPARENT Failure to Perform Post-Modification Testing for

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VIO

Control Room HVAC System (Apparent Violation).

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50-237/249-96014-02

VIO

Failure to Follow VETIP Procedure for Incoming

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Vendor Technical Information.

1

50-237/249-96014-03

URI

Battery Room Temporary Alteration.

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Closed

50-237:249/95010-03

VIO

Control of Overtime Not Implemented In

Accordance With Generic Letter (GL) 82-12.

50-237/249-95015-05

URI

Corner Room Steel.

50-237/249-96013-02

URI

Control Room Ventilation System Operability.

50-237/249-95008-01

IFI

Failure to Follow Procedure Resulted in Two

Inoperable Core Spray Systems.

50-237/249-95008-10

IFI

Emergency Lighting.

50-237:249/96002-04

IFI

Atmospheric Containment Atmosphere Dilution

(ACAD) Operating and Surveillance Procedures'

Bands Differ.

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LIST OF ACRONYM 3 USED

AC

Air Conditioning

i

ACAD

Atmospheric Containment Atmosphere Dilution

ALARA

As Low As Reasonably Achievable

CFR

Code of Federal Regulations

4

.

CRD

Coritrol Rod Drive

!

DAN

Dresden Annunciator Procedure

1

DAP

Dresden Administrative Procedure

DATR

Dresden Administrative Technical Requirements

4

DES

Dresden Electrical Surveillance

DFPS

Dresden Fire Protection Surveillance

DGP

Dresden General Procedure

2

DOA

Dresden Operating Abnormal

DOP

Dresden Operating Procedure

DOS

Dresden Operations Surveillance

dP

Differential Procedure

DTS

Dresden Technical Surveillance

a

EA

Enforcement Action

EDG

Emergency Diesel Generator

EPIP

Emergency Plan Implementing Procedures

-

ETI

Equipment Technical Information

FME

Foreign Material Exclusion

GL

Generic Letter

HPCI

High Pressure Coolant Injection

HVAC

Heating. Ventilation, and Air Conditioning

HVO

High Voltage Operator

"

IFI

Inspector Followup Item

ISI

Independent Safety Inspection

IWG

Inches Water Gage

,

'

LP

Low Pressure

MG

Motor Generator

MMD

Mechanical Maintenance Department

MWe

Megawatts Electrical

NEP

Nuclear Engineering Procedure

J

NDV

Notice of Violation

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PDR

Public Document Room

j

PIF

Performance Improvement Form

PORC

Plant Operations Review Committee

asig

Pounds Per Square Inch Gauge

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1R

Reactor Recirculation

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UFSAR

Updated Final Safety Analysis Report

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URI

Unresolved Item

VETIP

Vendor Equipment Technical Information Program

WEC

Work Execution Center

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