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                                              APPENDIX B
.
                                U.S. NUCLEAR REGULATORY COMMISSION
APPENDIX B
                                              REGION IV
U.S. NUCLEAR REGULATORY COMMISSION
        Inspection Report:     50-298/92-22               Operating License:   DPR-46
REGION IV
        Licensee:   Nebraska Public Power District
Inspection Report:
                    P.O. Box 499
50-298/92-22
                    Columbus, Nebraska     68602-0499
Operating License:
        Facility Name:     Cooper Nuclear Station
DPR-46
        Inspection At:     Brownville, Nebraska
Licensee:
        Inspection Conducted: October 4 through November 14, 1992
Nebraska Public Power District
        Inspectors:   R. A. Kopriva, Senior Resident Inspector
P.O. Box 499
                      W. C. Walker, Resident Inspector
Columbus, Nebraska
                      J. M. Keeton, Operator Licensing
68602-0499
      Approv '         #o                       yL                 2. _['1 '
Facility Name:
                          . Gagliardo,' liTeT7T jects section C       at
Cooper Nuclear Station
        Inspection Summar_y
Inspection At:
      Areas Inspected:     Routine, unannounced inspection of onsite response to
Brownville, Nebraska
      events, operational safety verification, surveillance observations, followup,
Inspection Conducted: October 4 through November 14, 1992
        and onsite review of licensee event reports.
Inspectors:
        Resulu:
R. A. Kopriva, Senior Resident Inspector
        e      Overall, the licensee operated the facility safety (paragraphs 2 and
W. C. Walker, Resident Inspector
              3.5).
J. M. Keeton, Operator Licensing
        *     The licensee's evaluation and corrective actions to address the water
Approv '
              hammer event in Residual Heat Removal System B on October 22,-1992, were
#o
              prompt and appeared to be good (paragraph 2),
yL
        o     Housekeeping was improving.     Licensee management was addressing this
2. _['1
                issue (paragraph 3.2).                                                 ;
. Gagliardo,' liTeT7T jects section C
        e      A compressed gas cylinder was not properly controlled on the refueling -
at
              floor for an extended period of time. This is a violation
'
                (paragraph 3.2),
Inspection Summar_y
        e      One example of improper control of visitors was identified. This is a
Areas Inspected:
              violation (paragraph 3.4).
Routine, unannounced inspection of onsite response to
        *     Surveillance tests were performed well. The licensee personnel involved
events, operational safety verification, surveillance observations, followup,
              were knowledgeable of the tasks required and their actions were good
and onsite review of licensee event reports.
                (paragraph 4.3).
Resulu:
      9212220245
Overall, the licensee operated the facility safety (paragraphs 2 and
        DR           921214
e
              ADOCK 05000298
3.5).
                            PDR
*
                                      ,           _       _
The licensee's evaluation and corrective actions to address the water
hammer event in Residual Heat Removal System B on October 22,-1992, were
prompt and appeared to be good (paragraph 2),
o
Housekeeping was improving.
Licensee management was addressing this
issue (paragraph 3.2).
;
A compressed gas cylinder was not properly controlled on the refueling -
e
floor for an extended period of time.
This is a violation
(paragraph 3.2),
One example of improper control of visitors was identified. This is a
e
violation (paragraph 3.4).
*
Surveillance tests were performed well.
The licensee personnel involved
were knowledgeable of the tasks required and their actions were good
(paragraph 4.3).
9212220245 921214
DR
ADOCK 05000298
PDR
,
_
_
.


                                                                        _.   _.
_.
    .
_.
  ..
.
..
.
.
+
+
                                            -2-
-2-
    *     The maintenance activity to repair and inspect the faulty diesel
*
            generator fuse holders was good (paragraph 5.1).
The maintenance activity to repair and inspect the faulty diesel
      s    The licensee appropriately addressed, from a safety perspective, the use
generator fuse holders was good (paragraph 5.1).
            of a process can in the spent fuel pool (paragraph 6.3).
The licensee appropriately addressed, from a safety perspective, the use
    *      Licensed operator training weaknesses were observed in command, control,
s
            and communications; however, the licensee was aware of the problems and
of a process can in the spent fuel pool (paragraph 6.3).
            was actively pursuing their corrective actions program. The simulator
Licensed operator training weaknesses were observed in command, control,
            evaluators were very professional and exhibited good evaluation skills.
*
            Examination material was very good and in accordance with the standard.
and communications; however, the licensee was aware of the problems and
            The licenset operators appeared to be safety-conscious and competent
was actively pursuing their corrective actions program.
            (paragraph 6.5).
The simulator
    Summar.y of Inspection Findings:
evaluators were very professional and exhibited good evaluation skills.
      e     Violation 298/9222-01 was opened (paragraph 3.2).
Examination material was very good and in accordance with the standard.
      e     Violation 298/9222-02 was opened (paragraph 3.4).
The licenset operators appeared to be safety-conscious and competent
      *     Inspection Followup Item 298/9034-02 was closed (paragraph 6.1).
(paragraph 6.5).
      e     Unresolved Item 298/9219-01 was closed (paragraph 6.2).
Summar.y of Inspection Findings:
      e     Unresolved Item 298/9219-02 was closed (paragraph 6.3).
e
      *     Licensee Event Reports 92-008, 92-012, and 92-013 were closed
Violation 298/9222-01 was opened (paragraph 3.2).
            (paragraph 7).
e
      Attachments (and/or Enclosures):
Violation 298/9222-02 was opened (paragraph 3.4).
      e   Attachment 1 - Persons Contacted and Exit Meeting
*
                    . - - - .
Inspection Followup Item 298/9034-02 was closed (paragraph 6.1).
e
Unresolved Item 298/9219-01 was closed (paragraph 6.2).
e
Unresolved Item 298/9219-02 was closed (paragraph 6.3).
*
Licensee Event Reports 92-008, 92-012, and 92-013 were closed
(paragraph 7).
Attachments (and/or Enclosures):
e
Attachment 1 - Persons Contacted and Exit Meeting
. - - - .


                                                              _- _             -.   _   .. _ _._.
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.. _ _._.
  ,
4
                                                    _3
I
                                              DETAILS
t
        1 PLANT STATUS                                                                           $
,
        At the beginning of this inspection period, the plant was operating at
_3
        53 percent power and in single-loop operation. On October 1, 1992, Reactor
DETAILS
        Recirculation Motor-Generator Set B had tripped due to a faulty resistor and
1 PLANT STATUS
        two faulty diodes. The components were replaced and the motor-generator set
$
        was restarted. The unit returned to full power on October 5. At the end of
At the beginning of this inspection period, the plant was operating at
        this inspection, the plant was operating at 100 percent power.
53 percent power and in single-loop operation. On October 1, 1992, Reactor
        2 ONSITE RESPONSE TO EVENT (93702)
Recirculation Motor-Generator Set B had tripped due to a faulty resistor and
                                                                                                  .
two faulty diodes.
        Residual Heat Removal System B Inoperable
The components were replaced and the motor-generator set
        On October 22, 1992, Residual Heat Removal System B was declared inoperable
was restarted.
        during performance of Surveillance Procedure 6.3.5.1, "RHR Test Mode
The unit returned to full power on October 5.
        Surveillance Operation Quarterly Inservice Test," Revision 35.
At the end of
        During the surveillance, Residual Heat Removal Pump B was run, determined to
this inspection, the plant was operating at 100 percent power.
        be acceptable, and shut down. Pump D was then aligned according to the
2 ONSITE RESPONSE TO EVENT (93702)
        procedure, which took approximately 5 minutes. Upon the starting of Pump D, a
.
        loud noise was heard. The licensee investigated the source of the noise and
Residual Heat Removal System B Inoperable
        located a leak on the 958 foot elevation of the reactor building, at the
On October 22, 1992, Residual Heat Removal System B was declared inoperable
                                        -
during performance of Surveillance Procedure 6.3.5.1, "RHR Test Mode
        flange for Pressure Maintenance System Check Valve 19. The check valve was
Surveillance Operation Quarterly Inservice Test," Revision 35.
        located in a 4-inch line which is part of the auxiliary ccndensate system,
During the surveillance, Residual Heat Removal Pump B was run, determined to
        which provides pressure maintena e o r the residual heat removal system.
be acceptable, and shut down.
        Approximately 50 gallons of wat e had leaked out of the system into the
Pump D was then aligned according to the
        reactor building. Licensee empsoyees bserved that the bonnet gasket on Check
procedure, which took approximately 5 minutes.
        Valve 19 was unseated. They pr3ce h to walk down the remainder of the
Upon the starting of Pump D, a
        pressure maintenance system and (Qsm ed two pipe supports which had been
loud noise was heard.
        deformed from-the event and als seve al pipe hangers which were misaligned.
The licensee investigated the source of the noise and
        The licensee determined that the n. <et faih re and pipe damage were caused by
located a leak on the 958 foot elevation of the reactor building, at the
        a water hammer.
-
        The licensee reviewed past water hammer events that have occurred in boiling
flange for Pressure Maintenance System Check Valve 19. The check valve was
        water reactors, conducted system walkdowns, and assov.ed the impact the water
located in a 4-inch line which is part of the auxiliary ccndensate system,
        hammer had on the residual heat removal system. The licensee repaired the
which provides pressure maintena e o r the residual heat removal system.
        pipe supports that were damaged and the check valve which was found to be
Approximately 50 gallons of wat e had leaked out of the system into the
I       leaking due to the ';ent. The check valve was functionally -tested and found
reactor building.
        to be satisfactory. Documentation was provided which showed that the event
Licensee empsoyees bserved that the bonnet gasket on Check
        had not compromised the system pressure boundary integrity in its repaired
Valve 19 was unseated.
        configuration.
They pr3ce h
        The licensee determined that the event was caused by valving out the pressure
to walk down the remainder of the
        maintenance system when switching over from Pump B to Pump D during the
pressure maintenance system and (Qsm ed two pipe supports which had been
        surveillance test. A procedure change had been made which requires that the
deformed from-the event and als seve al pipe hangers which were misaligned.
        pressure maintenance system remain in service during pump changeover. The
The licensee determined that the n.
L         inspectors reviewed the licensee's corrective actions and found them
<et faih re and pipe damage were caused by
a water hammer.
The licensee reviewed past water hammer events that have occurred in boiling
water reactors, conducted system walkdowns, and assov.ed the impact the water
hammer had on the residual heat removal system. The licensee repaired the
pipe supports that were damaged and the check valve which was found to be
I
leaking due to the ';ent.
The check valve was functionally -tested and found
to be satisfactory.
Documentation was provided which showed that the event
had not compromised the system pressure boundary integrity in its repaired
configuration.
The licensee determined that the event was caused by valving out the pressure
maintenance system when switching over from Pump B to Pump D during the
surveillance test.
A procedure change had been made which requires that the
pressure maintenance system remain in service during pump changeover.
The
L
inspectors reviewed the licensee's corrective actions and found them
appropriate.
!
!
          appropriate.
1
1
i.
i.
    -     _ . _ __  ._.         .         -   _ , , _ _ , .         . - _ _
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. - _
_


                    - _ - _ _ _ _ _ _ - _ .                                                         _
- _ - _ _ _ _ _ _ - _ .
_
l-
l-
                                                                                                      -4-
-4-
    Conclusions
Conclusions
    The licensee's evaluation and corrective actions were prompt and appeared to
The licensee's evaluation and corrective actions were prompt and appeared to
    be good.
be good.
    3 OPERATIONAL SAFETY VERIFICATION (71707)
3 OPERATIONAL SAFETY VERIFICATION (71707)
    3.1 Control Room Observations
3.1 Control Room Observations
    The inspectors observed operational activities throughout this inspection
The inspectors observed operational activities throughout this inspection
    period to verify that proper control room staffing and control room
period to verify that proper control room staffing and control room
    professionalism were maintained. Control room shift supervisor log book, tag
professionalism were maintained.
    out log book, and control room balance-of-plant log book entries were reviewed
Control room shift supervisor log book, tag
    to verify that appropriate entries were made. The licensee's control of these
out log book, and control room balance-of-plant log book entries were reviewed
    activities was good.
to verify that appropriate entries were made. The licensee's control of these
    3.2 Plant Tours
activities was good.
    The inspectors toured various areas of the plant to verify that proper
3.2 Plant Tours
    housekeeping was being maintained. Housekeeping was found to be improving,
The inspectors toured various areas of the plant to verify that proper
    but su4e areas remained where additional improvement was needed. The
housekeeping was being maintained.
      licensee's increased efforts for improving housekeeping were evident and
Housekeeping was found to be improving,
    management was continuing to review this activity.
but su4e areas remained where additional improvement was needed.
      On October 5, the inspectors found an unsecured, wheeled fire extinguisher in
The
      the reartor building on the 958-foot elevation and questioned the licensee as
licensee's increased efforts for improving housekeeping were evident and
      to what effect a seismic event would have on the unsecured fire extinguisher.
management was continuing to review this activity.
      Approximately 15 feet separated the fire extinguisher cart from Fuel Pool
On October 5, the inspectors found an unsecured, wheeled fire extinguisher in
      Cooling Instrument Rack 25-16 containing essential equipment. The licensee                         ;
the reartor building on the 958-foot elevation and questioned the licensee as
      performed a seismic analysis to determine whether the subject fire
to what effect a seismic event would have on the unsecured fire extinguisher.
      extinguisher could have interacted with essential equipment. The analysis
Approximately 15 feet separated the fire extinguisher cart from Fuel Pool
      concluded that it would be unlikei) that the extinguisher would topple during
Cooling Instrument Rack 25-16 containing essential equipment. The licensee
      a seismic event. However, if it did tip over, there was no essential
;
      eauipmerit located where it could interact with the extinguisher.
performed a seismic analysis to determine whether the subject fire
      As a conservative measure, the licensee secured the extinguisher. In
extinguisher could have interacted with essential equipment.
        addition, the licensee reviewed six other wheeled fire extinguisher locations
The analysis
      within the plant to determine possible interaction of those extinguisbers with
concluded that it would be unlikei) that the extinguisher would topple during
        essential equipment.                     The licensee concluded that no concerns existed with the
a seismic event. However, if it did tip over, there was no essential
        six other wheeled fire extinguishers. The inspectors reviewed the licensee's
eauipmerit located where it could interact with the extinguisher.
        actions and considered them to be appropriate.
As a conservative measure, the licensee secured the extinguisher.
        On October 6,1992, during a walkdown of the reactor building, the inspector
In
        identified a gas cylinder in the northwest quadrant of the refueling floor                         j
addition, the licensee reviewed six other wheeled fire extinguisher locations
        which was roped to the two-wheel cart used for transporting the gas cylinder.
within the plant to determine possible interaction of those extinguisbers with
        The gas cylinder was not secured to a fixed restraint, the cart was not a
essential equipment.
        wheeled cart of approved design for storage or use, and the wheels of the cart
The licensee concluded that no concerns existed with the
        were not blocked or locked. At the time of discovery the inspector could not
six other wheeled fire extinguishers. The inspectors reviewed the licensee's
        identify a use for the cylinder or the status of the cylinder (i.e., whether
actions and considered them to be appropriate.
                                                                                                            I
On October 6,1992, during a walkdown of the reactor building, the inspector
                                                                                                              1
identified a gas cylinder in the northwest quadrant of the refueling floor
  _                                       ___ _ _____ _ _ _ _ __________ __.___ ____ _ _ _ _ _ __
j
which was roped to the two-wheel cart used for transporting the gas cylinder.
The gas cylinder was not secured to a fixed restraint, the cart was not a
wheeled cart of approved design for storage or use, and the wheels of the cart
were not blocked or locked. At the time of discovery the inspector could not
identify a use for the cylinder or the status of the cylinder (i.e., whether
I
1
_
___ _ _____ _ _ _ _ __________ __.___ ____ _ _ _ _ _ __


                                                                                                        ~
~
.. .
..
                                                                                                        !
.
                                          _S.
!
  it was full or empty). Under certain conditions, the cylinder could become a
_S.
  missile and damage equipment or personnel on the refueling floor or equipment                       l
it was full or empty). Under certain conditions, the cylinder could become a
  in the fuel pool.                                                                                   ;
missile and damage equipment or personnel on the refueling floor or equipment
  The licensee determined that the gas cylinder was helium and that it had been
l
  used on April 11 to leak test the reactor pressure vessel . surveillance
in the fuel pool.
  specimen shipping cask in accordance with Special Procedure 92-022. The
;
  special procedure did not include specific precautions or instructions for-
The licensee determined that the gas cylinder was helium and that it had been
  handling, storage, or removal of the gas cylinder- The licensee removed the                           .
used on April 11 to leak test the reactor pressure vessel . surveillance
  gas cylinder from the refueling floor. The protective cap was in place on the
specimen shipping cask in accordance with Special Procedure 92-022.
  cylinder and it was partially, if not completely, depressurized.
The
  Title 10 CFR Part 50, Appendix B, Criterion V, states that activities
special procedure did not include specific precautions or instructions for-
  affecting quality shall be prescribed by documented instruction, 3rocedures,
handling, storage, or removal of the gas cylinder- The licensee removed the
                                                                    .
.
  or drawings of a type appropriate to the circumstances and shall ae
gas cylinder from the refueling floor.
  accomplished in accordance with these instructions, procedures, or drawings.
The protective cap was in place on the
  Procedure 0.7, Revision 8, " Flammable, Combustible, and Chemical Material
cylinder and it was partially, if not completely, depressurized.
  Control," paragraph-8.3.2.2.0, states that, during storage and use, gas
Title 10 CFR Part 50, Appendix B, Criterion V, states that activities
  cylinders shall be individually secured to a fixed suppor.t by a restraint, and
affecting quality shall be prescribed by documented instruction,
  paragraph 8.3.2.3 states that use of wheel-mounted carts of approved design
3rocedures,
  are permitted for certain uses of gas cylinders. .The helium gas cylinder had
.
  been on the refueling floor since approximately April 11 and on October 6 was
or drawings of a type appropriate to the circumstances and shall
  not secured to a fixed support and was not on a wheel-mounted cart of approved
ae
  design.   This is a violation.(298/9222-01).
accomplished in accordance with these instructions, procedures, or drawings.
  3.3 Radiological Protection Observations
Procedure 0.7, Revision 8, " Flammable, Combustible, and Chemical Material
  The inspectors verified that selected radiological protection activities were
Control," paragraph-8.3.2.2.0, states that, during storage and use, gas
  in conformance with facility policies, procedures, and regulatory
cylinders shall be individually secured to a fixed suppor.t by a restraint, and
  requirements. Radiation and/or contaminated areas were properly posted and
paragraph 8.3.2.3 states that use of wheel-mounted carts of approved design
  controlled.
are permitted for certain uses of gas cylinders. .The helium gas cylinder had
  3.4 Security Program Observations
been on the refueling floor since approximately April 11 and on October 6 was
  On October 5, the inspectors observed a repairman, with a visitor's badge, on
not secured to a fixed support and was not on a wheel-mounted cart of approved
  the_ first floor of the administration building, in a room with two separate
design.
  access points, and he was not within the line of sight of his escort.     One
This is a violation.(298/9222-01).
  access point would have allowed the repairman to leave the-work area-unseen by                       !
3.3 Radiological Protection Observations
                                                                                                        "
The inspectors verified that selected radiological protection activities were
  the escort and obtain access to other areas within the protected area. ..The-
in conformance with facility policies, procedures, and regulatory
  inspectors asked the repairman about his escort. The repairman thought he
requirements. Radiation and/or contaminated areas were properly posted and
  could identify his escort, but was uncertain where the escort was. The
controlled.
  inspectors located the escort. The escort had assumed that the access door
3.4 Security Program Observations
  leading from the work room to other areas within the plant was closed. After                       o
On October 5, the inspectors observed a repairman, with a visitor's badge, on
  being questioned by the inspectors,=the door was closed. However, there was                           ,
the_ first floor of the administration building, in a room with two separate
  no way to lock this door which would prevent the repairman from exiting                               :
access points, and he was not within the line of sight of his escort.
  unobserved. The inspectors promptly reported the situation ~to station                                 !
One
  security and a security officer was dispatched to review the situation.                               l
access point would have allowed the repairman to leave the-work area-unseen by
  The inspectors reviewed the licensee's escort training and training
!
  documentation. The escort training lesson plan and Visitor / Tour Station                             l
"
                                                                                                          1
the escort and obtain access to other areas within the protected area. ..The-
                                                                                                          I
inspectors asked the repairman about his escort. The repairman thought he
                                                                                                          l
could identify his escort, but was uncertain where the escort was. The
                                                                                                          1
inspectors located the escort. The escort had assumed that the access door
                                                                          -     - - . - _ , _ - . , ,
leading from the work room to other areas within the plant was closed. After
o
being questioned by the inspectors,=the door was closed.
However, there was
,
no way to lock this door which would prevent the repairman from exiting
:
unobserved. The inspectors promptly reported the situation ~to station
security and a security officer was dispatched to review the situation.
l
The inspectors reviewed the licensee's escort training and training
documentation.
The escort training lesson plan and Visitor / Tour Station
1
1
-
- - . - _ , _ - . , ,


_ _ _ _ _           _ _           __ _ . - _ _ _ _ _ _.                           ._ _ _ _ ._ _ _ .
_ _ _ _ _
      .         .
_ _
                                                                    -6-
__ _ . - _ _ _ _ _ _.
              Access Procedure 1.15 provided instructions to escorts to maintain positive
._ _ _ _ ._ _ _ .
              control of visitors. The individual responsible for escorting the repairman
.
              had received the training. The licensee counseled the individual responsible
.
              for escorting the visitor to ensure understanding of proper escort procedures,
-6-
              On October 5, Security Event Report 92-224 was completed, which outlined the
Access Procedure 1.15 provided instructions to escorts to maintain positive
              event details. immediate corrective actions included providing an escort for
control of visitors.
              the repairman and sending a security guard to the incident location to review
The individual responsible for escorting the repairman
              the situation. The licensee also counselled the individual, emphasizing
had received the training. The licensee counseled the individual responsible
              instructions regarding visitor control requirements. The licensee was
for escorting the visitor to ensure understanding of proper escort procedures,
              reviewing the procedures to determine their adequacy, and long-ierm corrective
On October 5, Security Event Report 92-224 was completed, which outlined the
              actions had not been established at the end of this report period.
event details.
              Title 10 CFR 50.34(c) requires that each application for a license to operate
immediate corrective actions included providing an escort for
              a production or utilization facility shall include a physical security plan.
the repairman and sending a security guard to the incident location to review
              The Cooper Nuclear Station Physical Security Plan, Section 1.5.2, requires
the situation.
              that escorts exercise and maintain control of their visitors at all times.
The licensee also counselled the individual, emphasizing
              Cooper- Nuclear Station Operations Manual, Plant Services Procedure 1.15,                                 ,
instructions regarding visitor control requirements. The licensee was
              " Visitor / Tour Station Access," Revision 8, Section 4.2.1, states that an
reviewing the procedures to determine their adequacy, and long-ierm corrective
              escort is responsible to exercise and maintain control of the visitor at all
actions had not been established at the end of this report period.
              times,       The failure to exercise and maintain control of a visitor (i.e., an
Title 10 CFR 50.34(c) requires that each application for a license to operate
              individual not authorized by the licensee to enter protected areas without an
a production or utilization facility shall include a physical security plan.
              escort) while the visitor was working within the protected area on October 5,
The Cooper Nuclear Station Physical Security Plan, Section 1.5.2, requires
              1992, is a violation of NRC requirements (298/9222-02).
that escorts exercise and maintain control of their visitors at all times.
              3.5 Conclusions
Cooper- Nuclear Station Operations Manual, Plant Services Procedure 1.15,
              *          Overall, the licensee operated the facility safely,
,
              *         Housekeeping was improving.         Licensee management was addressing this
" Visitor / Tour Station Access," Revision 8, Section 4.2.1, states that an
                        issue.
escort is responsible to exercise and maintain control of the visitor at all
              *          A compressed gas cylinder was not properly controlled on the refueling
times,
                        floor for an extended period of time. This is a violation.
The failure to exercise and maintain control of a visitor (i.e., an
              *          One example _of- improper control of visitors was identified. This is a
individual not authorized by the licensee to enter protected areas without an
                        violation.
escort) while the visitor was working within the protected area on October 5,
            -4     SURVEILLANCE 0BSERVATIONS (61726)
1992, is a violation of NRC requirements (298/9222-02).
              4.1 Undervoltage Relays and Rela _y Timers Functional Test
3.5 Conclusions
              On October 16, 1992, the inspector observed the performance of Surveillance-
Overall, the licensee operated the facility safely,
              Procedure 6.2.2.1.10. "4160V Buses If and 1G Undervoltage Relays and Relay
*
              Timers Functional Test," Revision 18.
*
                                                                                                                        '
Housekeeping was improving.
              Operators appeared to be following the surveillance procedure both locally and
Licensee management was addressing this
              in the control room. Good communications were noted between the control room
issue.
              operators and individuals performing the surveillance. In reviewing the
A compressed gas cylinder was not properly controlled on the refueling
    . - - .     .,       -..           .       -..   -, . . . - .     - . - - -           .-     _.- -.-. . . . -
*
floor for an extended period of time.
This is a violation.
One example _of- improper control of visitors was identified.
This is a
*
violation.
-4
SURVEILLANCE 0BSERVATIONS (61726)
4.1 Undervoltage Relays and Rela _y Timers Functional Test
On October 16, 1992, the inspector observed the performance of Surveillance-
Procedure 6.2.2.1.10. "4160V Buses If and 1G Undervoltage Relays and Relay
Timers Functional Test," Revision 18.
Operators appeared to be following the surveillance procedure both locally and
'
in the control room.
Good communications were noted between the control room
operators and individuals performing the surveillance.
In reviewing the
. - - .
.,
-..
.
-..
-,
. . . - .
- . - - -
.-
.- -.-. . . . -


              ,- -
,- -
                                                                                      3
3
  ,
.
    .  .
.
                                                                                      -;
,
                                                                                      ,
-;
  .
,
                                            -7-                                         .
.
                                                                                        )
-7-
      procedures the inspector noted that proper signatures and approvals were         .
.
                                                                                      ~
)
      evident. During the surveillance the inspector observed that the conditions
procedures the inspector noted that proper signatures and approvals were
      inside the 4160V breaker cabinets were clean.                                   ;
.
      4.2 Reactor Core isolation Coolina Steam line Hiah Flow Calibration and
~
            Functional Test
evident.
      On October 28 the inspectors observed performance of Surveillance
During the surveillance the inspector observed that the conditions
inside the 4160V breaker cabinets were clean.
;
4.2 Reactor Core isolation Coolina Steam line Hiah Flow Calibration and
Functional Test
On October 28 the inspectors observed performance of Surveillance
Procedure 6.2.2.6.1 " Reactor Core Isolation Cooling Steam Line High Flow
Calibration and Functional Test," Revision 21. The inspector observed an-
'
'
      Procedure 6.2.2.6.1 " Reactor Core Isolation Cooling Steam Line High Flow
instrument mechanic performing the calibration of the differential pressure
      Calibration and Functional Test," Revision 21. The inspector observed an-
switches which are used to monitor reactor core isolation cooling steam line
      instrument mechanic performing the calibration of the differential pressure
fl ow. The instrument mechanic was adhering to the procedure and-m..intained
      switches which are used to monitor reactor core isolation cooling steam line
good communications with the control room operators-throughout the
      fl ow. The instrument mechanic was adhering to the procedure and-m..intained
surveillance.
      good communications with the control room operators-throughout the
The instrument mechanic was conscientious in complying with
      surveillance. The instrument mechanic was conscientious in complying with
good radiological practice as he routinely changed protective gloves during
      good radiological practice as he routinely changed protective gloves during
his manipulation of the valves associated with the differential pressure
      his manipulation of the valves associated with the differential pressure
switches.
      switches. The surveillance was completed satisfactorily with no anomalies
The surveillance was completed satisfactorily with no anomalies
      encountered.
encountered.
      4.3 Conclusions
4.3 Conclusions
      The surveillances observed were performed well. The licensee personnel:
The surveillances observed were performed well.
      involved were knowledgeable of the tasks required and executed these tasks
The licensee personnel:
      sufficiently to comply with the procedures. The inspectors found the licensee
involved were knowledgeable of the tasks required and executed these tasks
      actions, as they pertained to these surveillances, to be good,
sufficiently to comply with the procedures. The inspectors found the licensee
      5 MAINTENANCE OBSERVATION (62703)
actions, as they pertained to these surveillances, to be good,
      On November 10, 1992, during a routine surveillance run of Emergency Diesel
5 MAINTENANCE OBSERVATION (62703)
      Generator 1, it was noted that.the air start solenoid to_one bank of air
On November 10, 1992, during a routine surveillance run of Emergency Diesel
      cylinders had not actuated. Upon'further investigation, the licensee found
Generator 1, it was noted that.the air start solenoid to_one bank of air
      the fuse holder for that solenoid to be loose.
cylinders had not actuated.
      The inspectors observed the corrective: maintenance activity to repair the fuse
Upon'further investigation, the licensee found
      holder and the panel inspections-to check other fuse holders that may have-
the fuse holder for that solenoid to be loose.
      experienced similar problems. The licensee did not -identify any addition
The inspectors observed the corrective: maintenance activity to repair the fuse
      examples.of this deficiency. The inspectors verified ~that the workers           *
holder and the panel inspections-to check other fuse holders that may have-
      obtained proper authorization to perform the work, _that control room operators
experienced similar problems. The licensee did not -identify any addition
      were cognizant.of the maintenance activity, that workers followed'the
*
      maintenance instructions, and that appropriate safety. precautions were taken
examples.of this deficiency. The inspectors verified ~that the workers
      for work in energized panels. The inspector observed the postmaintenance
obtained proper authorization to perform the work, _that control room operators
      functional check of the solenoid and verified proper operation. The
were cognizant.of the maintenance activity, that workers followed'the
      inspectors noted that the electrical cabinets were clean. No unacceptable-
maintenance instructions, and that appropriate safety. precautions were taken
.    conditions were identified.
for work in energized panels. The inspector observed the postmaintenance
      5.1 Conclusion
functional check of the solenoid and verified proper operation.
      The maintenance activity to repair and inspect _ i -   >olders was good.
The
inspectors noted that the electrical cabinets were clean.
No unacceptable-
conditions were identified.
.
5.1 Conclusion
The maintenance activity to repair and inspect _ i -
>olders was good.
l
l
,
,
              e         v
e
v


                                                                -             ..     - ,
-
  .
..
-
,
.
.
.
,
,
                                            -8-
-8-
    6 FOLLOWUP (92701)
6 FOLLOWUP (92701)
    6.1   (Closed) Inspection Followup Item 298/9034-02: Entry into a Technical
6.1
          Specification Limittna Condition for Operation During the Performance of
(Closed) Inspection Followup Item 298/9034-02:
          Surveillance Testing
Entry into a Technical
    The resident inspectors reviewed a licensee memorandum dated April 17, 1991,
Specification Limittna Condition for Operation During the Performance of
    which outlined proposed technical guidance and reflected existing policy on
Surveillance Testing
    the subject of entering Technical Specification. action statements during the
The resident inspectors reviewed a licensee memorandum dated April 17, 1991,
    performance of surveillance testing. The licensee had identified several
which outlined proposed technical guidance and reflected existing policy on
    cases where procedures could disable a safety function during the performance
the subject of entering Technical Specification. action statements during the
    of a routine test. As a result, several procedures were revised.       Certain
performance of surveillance testing.
    Technical Specification surveillance requirements have been amended to change
The licensee had identified several
    the test frequency to allow the performance of the st/veillance procedures
cases where procedures could disable a safety function during the performance
    during refueling shutdowns instead of performing these at power.- Also, a
of a routine test.
    Technical Specification amendment eliminated the testing of certain systems
As a result, several procedures were revised.
    and components following the failure of a redundant system or component, a
Certain
    practice which could result in the removal from service of the only operable
Technical Specification surveillance requirements have been amended to change
    system or component. The licensee has taken further action to address the
the test frequency to allow the performance of the st/veillance procedures
    issue of operability during the performance of surveillance procedures by
during refueling shutdowns instead of performing these at power.- Also, a
    organizing a task force to identify additional required changes in the
Technical Specification amendment eliminated the testing of certain systems
    surveillance program and Technical Specifications.
and components following the failure of a redundant system or component, a
    6.2 _(Closed) Unresolved Item 298/9219-01:     Implementina Organizational Change
practice which could result in the removal from service of the only operable
          without Having Amended the Technical Specifications
system or component. The licensee has taken further action to address the
    The licensee implemented a site reorganization on July 20, 1992, and had not
issue of operability during the performance of surveillance procedures by
    revised their Technical Specifications to reflect the changes in the
organizing a task force to identify additional required changes in the
    reorganization.   On October 8, the licensee submitted their-Technical
surveillance program and Technical Specifications.
    Specification amendment to the Commission. Inspectors reviewed, for the time
6.2 _(Closed) Unresolved Item 298/9219-01:
    between reorganization and submittal of the amendment, the person assigned
Implementina Organizational Change
    full. time responsibility for the operation of the facility as specified in
without Having Amended the Technical Specifications
    Technical Specification 6.1.1. The inspectors concluded that the licensee met
The licensee implemented a site reorganization on July 20, 1992, and had not
    Technical Specification 6.1.1 during this time period.
revised their Technical Specifications to reflect the changes in the
    6.3 LClosed) Unresolved item 298/9219-02:     Potential Failure to Perform a
reorganization.
          10 CFR 50.59 Review for Eauipraent Placed on Ten of Empty Spent Fuel Racks
On October 8, the licensee submitted their-Technical
    On September 25, 1992, during a plant walkdown, the inspector identified a
Specification amendment to the Commission.
    process can located on top of empty spent fuel racks. The process can was
Inspectors reviewed, for the time
    used as part of the licensee's spent fuel pool cleanup project. The
between reorganization and submittal of the amendment, the person assigned
    inspectors questioned whether a 10 CFR 50.59-evaluation for the process can
full. time responsibility for the operation of the facility as specified in
    pertaining to its location on the spent fuel racks had been performed.
Technical Specification 6.1.1.
    The process can was 2 feet in diameter by 4 feet long with a fully loaded
The inspectors concluded that the licensee met
    weight of.approximately 800 pounds. An engineering evaluation had been
Technical Specification 6.1.1 during this time period.
    performed prior to placement of the can on the spent fuel racks, to ensure
6.3 LClosed) Unresolved item 298/9219-02:
    that the racks would handle the fully loaded weight of the can. Also, the
Potential Failure to Perform a
    licensee considered the possibility of damaging fuel assemblies should a
10 CFR 50.59 Review for Eauipraent Placed on Ten of Empty Spent Fuel Racks
    seismic event or industrial accident happen. Interaction between the can and
On September 25, 1992, during a plant walkdown, the inspector identified a
process can located on top of empty spent fuel racks.
The process can was
used as part of the licensee's spent fuel pool cleanup project.
The
inspectors questioned whether a 10 CFR 50.59-evaluation for the process can
pertaining to its location on the spent fuel racks had been performed.
The process can was 2 feet in diameter by 4 feet long with a fully loaded
weight of.approximately 800 pounds. An engineering evaluation had been
performed prior to placement of the can on the spent fuel racks, to ensure
that the racks would handle the fully loaded weight of the can.
Also, the
licensee considered the possibility of damaging fuel assemblies should a
seismic event or industrial accident happen.
Interaction between the can and


    '
'
  ,
,
  s
s
                                            -9-
-9-
                                                                                                  ,
,
    spent fuel assemblies was not deemed to be credible _because of the 20-foot
spent fuel assemblies was not deemed to be credible _because of the 20-foot
    distance between the can and the storage racks containing spent fuel.
distance between the can and the storage racks containing spent fuel.
    The licensee concluded that the calculated design basis seismic force would
The licensee concluded that the calculated design basis seismic force would
    overcome the friction between the process can and the spent fuel rack before
overcome the friction between the process can and the spent fuel rack before
    tipping the can, therefore, the can would remain upright-and horizontal
tipping the can, therefore, the can would remain upright-and horizontal
    movement would be limited because of the oscillating nature of a seismic
movement would be limited because of the oscillating nature of a seismic
    event. lhe can was submerged in water which had a dampening effect on any
event.
    movement of the can. If the process can were to slice or roll far enough to
lhe can was submerged in water which had a dampening effect on any
    impact fuel bundles, damage to the fuel assemblies would not be expected. The
movement of the can.
    fuel manufacturer estimated that it would take 250 foot-pounds of downward
If the process can were to slice or roll far enough to
    impact loading to damage one fuel rod. further, the licensee's_ Refuel
impact fuel bundles, damage to the fuel assemblies would not be expected.
    Accident Radiological Effects Calculation (No, NEDC 88-171), which assumes
The
    111 rods to be broken, concludes that the resulting lifetime-thyroid and whole
fuel manufacturer estimated that it would take 250 foot-pounds of downward
    body dose would be less than 1 percent of the NRC 10 CFR Part 100 reactor
impact loading to damage one fuel rod.
    siting criteria. The relationship between a vertical drop loading and a side
further, the licensee's_ Refuel
    loading (assuming the process can moves horizontally) would not be one to one.
Accident Radiological Effects Calculation (No, NEDC 88-171), which assumes
    The 800 pound process can would have to free-fall approximately 34 feet- to
111 rods to be broken, concludes that the resulting lifetime-thyroid and whole
    damage 111 fuel rods. This amount of energy would not be attainable for the
body dose would be less than 1 percent of the NRC 10 CFR Part 100 reactor
    configuration and controls the licensee had in place for the process can. If
siting criteria. The relationship between a vertical drop loading and a side
    the can were to move in a direction away from the spent fuel, it could
loading (assuming the process can moves horizontally) would not be one to one.
    possibly fall into the cask pad area of the fuel pool. This accident would be
The 800 pound process can would have to free-fall approximately 34 feet- to
    significantly less severe than the shipping cask drop accident analyzed in
damage 111 fuel rods.
    Burns & Roe Calculation 2520-02.
This amount of energy would not be attainable for the
    Concerns for loose parts-(i.e., if the can were to topple over) falling into
configuration and controls the licensee had in place for the process can.
    the spent fuel pool or even potentially being transported into the reactor
If
    have been addressed in bounding analysis previously completed for the site.
the can were to move in a direction away from the spent fuel, it could
    The licensee concluded that, with the procedures being used, the location of
possibly fall into the cask pad area of the fuel pool.
    the process can in the spent fuel pool, and the previous analysis performed,
This accident would be
    all safety questions / concerns pertaining to the process can had been
significantly less severe than the shipping cask drop accident analyzed in
    addressed.
Burns & Roe Calculation 2520-02.
    The inspectors concluded that the licensee's evaluation of the use of the
Concerns for loose parts-(i.e., if the can were to topple over) falling into
    process can was appropriate.
the spent fuel pool or even potentially being transported into the reactor
    6.4 Licensed Operator Requalification Program Evaluation
have been addressed in bounding analysis previously completed for the site.
                                                                                                  ?
The licensee concluded that, with the procedures being used, the location of
                                                                                                  *
the process can in the spent fuel pool, and the previous analysis performed,
    On November 4 and 5, 1992, the resident inspector and a Region-based inspector
all safety questions / concerns pertaining to the process can had been
    observed some requalification examinations, interviewed on-shift' supervisors,
addressed.
    and reviewed training and testing material. . Also, the licensed operators were
The inspectors concluded that the licensee's evaluation of the use of the
    observed during the simulator examinations to determine if they were
process can was appropriate.
    conducting activities in a manner conducive to protection of the public health
6.4 Licensed Operator Requalification Program Evaluation
    and safety.
?*
On November 4 and 5, 1992, the resident inspector and a Region-based inspector
observed some requalification examinations, interviewed on-shift' supervisors,
and reviewed training and testing material. . Also, the licensed operators were
observed during the simulator examinations to determine if they were
conducting activities in a manner conducive to protection of the public health
and safety.
l
l
    The following previously identified weaknesses (from NRC Inspection
The following previously identified weaknesses (from NRC Inspection
Report 50-298/9102) were specifically addressed either by direct observation,
'
'
    Report 50-298/9102) were specifically addressed either by direct observation,
interviews, or by reviewing training program records:
      interviews, or by reviewing training program records:
-
                                                -               .   .   --   _ . _ ___ _ _ _ _ _
.
.
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  .
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.
                                          -10-
.
  e     Crew command, control, and communication
-10-
  e     Adequacy of simulator scenarios
e
  e      Operators' ability to establish shutdown cooling
Crew command, control, and communication
  e     Operators' ability to diagnose conditions
e
  Some communications weaknesses were seen during this inspection:
Adequacy of simulator scenarios
  e      During one scenario, the supervisor directing panel activities was not
Operators' ability to establish shutdown cooling
        concise in his directives. A lack of uniformity in communication among
e
        crews was seen,
Operators' ability to diagnose conditions
  o      During another scenario, a supervisor directed an operator to establish
e
        torus spray. The operator could not get torus spray started and did not
Some communications weaknesses were seen during this inspection:
        inform the supervisor, who assumed that the torus was being sprayed.
During one scenario, the supervisor directing panel activities was not
  The communications problems observed were compensated by actions of the
e
  operators such that safety problems did not develop and mitigation strategies
concise in his directives. A lack of uniformity in communication among
  were not degraded. The facility managers stated that initiatives were in
crews was seen,
  progress to improve communications. This was primarily being done in the
During another scenario, a supervisor directed an operator to establish
  evaluation sessions during the requalification training. There was no formal
o
  classroom presentation geared to defining a communications policy.
torus spray.
  Training Guide NTG 318, " Command and Control" and operations directive, "CNS
The operator could not get torus spray started and did not
  Communications," were developed to address command and control. However,
inform the supervisor, who assumed that the torus was being sprayed.
  there did not appear to be a formal method to define -their interrelationship.
The communications problems observed were compensated by actions of the
  Command and control training had been incorporated into the evaluation
operators such that safety problems did not develop and mitigation strategies
  sessions during requalification training, but there were no formal classroom
were not degraded. The facility managers stated that initiatives were in
  presentations scheduled to address this area.
progress to improve communications.
  A review of the training and testing material used for this requalification
This was primarily being done in the
  cycle showed that the material was current-and that mechanisms were in place
evaluation sessions during the requalification training.
  to update the material. The simulator scenarios developed for this. evaluation
There was no formal
  were in accordance with the guidelines stated in NUREG-1021, " Operator-
classroom presentation geared to defining a communications policy.
  L.icensing Examiner Standards," Revision 7. Critical task identification and
Training Guide NTG 318, " Command and Control" and operations directive, "CNS
  task standard definitions were very good. A review of the graded written-
Communications," were developed to address command and control.
  examinations indicated that they were developed based on the sample-plan' and
However,
  that they discriminated at the proper level.
there did not appear to be a formal method to define -their interrelationship.
  During the simulator scenarios and walkthroughs, conditions existed that
Command and control training had been incorporated into the evaluation
  required establishing shutdown cooling. The operators were able to perform
sessions during requalification training, but there were no formal classroom
  all operations necessary to ' accomplish shutdown cooling. No errors were
presentations scheduled to address this area.
  noted.
A review of the training and testing material used for this requalification
  The licensed operators observed during the simulator and walkthrough
cycle showed that the material was current-and that mechanisms were in place
  examinations demonstrated the ability to diagnose events and conditions.   No.
to update the material.
  errors were observed.
The simulator scenarios developed for this. evaluation
  The facility evaluators conducted the dynamic simulator and walkthrough
were in accordance with the guidelines stated in NUREG-1021, " Operator-
  examinations professionally and in accordance with the standards. The
L.icensing Examiner Standards," Revision 7.
Critical task identification and
task standard definitions were very good.
A review of the graded written-
examinations indicated that they were developed based on the sample-plan' and
that they discriminated at the proper level.
During the simulator scenarios and walkthroughs, conditions existed that
required establishing shutdown cooling.
The operators were able to perform
all operations necessary to ' accomplish shutdown cooling.
No errors were
noted.
The licensed operators observed during the simulator and walkthrough
examinations demonstrated the ability to diagnose events and conditions.
No.
errors were observed.
The facility evaluators conducted the dynamic simulator and walkthrough
examinations professionally and in accordance with the standards.
The


                                    .   -         -     .   -               .
.
    .
-
.                                                                                 ,
-
                                                                                    I
.
-
.
.
.
,
I
..
..
                                          -11-
-11-
  evaluators were able to function autonomously without management interference
evaluators were able to function autonomously without management interference
  or visible constraints. During simulator evaluation sessions that were           ,
or visible constraints. During simulator evaluation sessions that were
  observed, the lead examiner elicited full participation from all evaluators.
,
  Facility evaluations were consistent with their program guidance, and the
observed, the lead examiner elicited full participation from all evaluators.
  licensee took appropriate measures to preserve examination integrity.
Facility evaluations were consistent with their program guidance, and the
  Other observations made by the inspectors and connunicated to the licensee
licensee took appropriate measures to preserve examination integrity.
  include:
Other observations made by the inspectors and connunicated to the licensee
  e     Shift technical advisor rotation policy and involvement during
include:
          requalification examinations was not fully understood by the shift
e
          Crews.
Shift technical advisor rotation policy and involvement during
  e      Simulator difficultly with P-1 printout has contributed to negative
requalification examinations was not fully understood by the shift
          training.   Rather than following up when a P-1 was not obtained, the
Crews.
          crew assumed it was a simulator problem and simulated having a. printout.
Simulator difficultly with P-1 printout has contributed to negative
  *      At one point during a shift crew scenario, both reactor operators were
e
          behind the control panels at the same time.
training.
  e      Based on inspectors' observations, the licensee has made progress to
Rather than following up when a P-1 was not obtained, the
          increase operations' sense of ownership in training.
crew assumed it was a simulator problem and simulated having a. printout.
  Areas of strength that were identified include:
At one point during a shift crew scenario, both reactor operators were
  *      Evaluators were very professional and exhibited good evaluation skills,
*
  o      Examination material was very good and in accordance with the standard.-
behind the control panels at the same time.
  *      Licensed operators took a serious professional approach to the annual
Based on inspectors' observations, the licensee has made progress to
          evaluation.
e
  Although weaknesses were seen in command, control, and communications, the
increase operations' sense of ownership in training.
  licensee was aware of the problems and was actively pursuing their corrective
Areas of strength that were identified include:
  actions program. The licensed operators appeared to be' safety-conscious and
Evaluators were very professional and exhibited good evaluation skills,
  competent.
*
  6.5 Conclusions
Examination material was very good and in accordance with the standard.-
    e    The licensee appropriately addressed, from a safety perspective, the use
o
          of a process can in the spent fuel pool.
Licensed operators took a serious professional approach to the annual
    *    Licensed operator training weaknesses were observed in command, control,
*
          and communications; however, the licensee was aware of the problems and
evaluation.
          was actively pursuing their corrective actions program. The simulator
Although weaknesses were seen in command, control, and communications, the
          evaluators were very professional and exhibited good evaluation skills.
licensee was aware of the problems and was actively pursuing their corrective
          Examination material was very good and in accordance with the standard.
actions program.
          The licensed operators appeared to be safety-conscious and competent.
The licensed operators appeared to be' safety-conscious and
competent.
6.5 Conclusions
The licensee appropriately addressed, from a safety perspective, the use
e
of a process can in the spent fuel pool.
Licensed operator training weaknesses were observed in command, control,
*
and communications; however, the licensee was aware of the problems and
was actively pursuing their corrective actions program. The simulator
evaluators were very professional and exhibited good evaluation skills.
Examination material was very good and in accordance with the standard.
The licensed operators appeared to be safety-conscious and competent.


,
,
                                                                                          .;
. ;
    ,-- .
, - -
  .
.
  .
.
                                                -12-
.
        7 ONSITE REVIEW 0F LICENSEE EVENT REPORTS (92700)
-12-
        7.1   (Closed) Licensee Event Report 298/92-008: Inoperability of the High
7 ONSITE REVIEW 0F LICENSEE EVENT REPORTS (92700)
              Pressure Coolant Injection System Due to Stem Nut Wear of a Motor-
7.1
              Operated Valve
(Closed) Licensee Event Report 298/92-008:
        This licensee event report documented the licensee's determination that the
Inoperability of the High
        high pressure coolant injection valve, HPCI-MOV-58, which is the pump suction
Pressure Coolant Injection System Due to Stem Nut Wear of a Motor-
        valve from the torus, was not stroking properly. During the running of
Operated Valve
        Surveillance Procedure 6.2.2.3.4, "HPCI Suppression Chamber and Emergency
This licensee event report documented the licensee's determination that the
        Condensate Storage Tank Water Level Calibration and Functional / Functional Test
high pressure coolant injection valve, HPCI-MOV-58, which is the pump suction
        and Water Initiation," Revision 25, both HPCI-MOV-58 and HPCI-MOV-17,-the pump
valve from the torus, was not stroking properly.
        suction valve from the emergency condensate storage tank, could have been
During the running of
        closed. The system logic for these two valves is such that one of them should
Surveillance Procedure 6.2.2.3.4, "HPCI Suppression Chamber and Emergency
        always remain in an open position to provide suction for emergency core
Condensate Storage Tank Water Level Calibration and Functional / Functional Test
        cooling through the high pressure coolant injection system.
and Water Initiation," Revision 25, both HPCI-MOV-58 and HPCI-MOV-17,-the pump
        The licensee concluded that, had the high pressure coolant injection system
suction valve from the emergency condensate storage tank, could have been
        been required, it would have functioned as designed for as long as 10 minutes
closed. The system logic for these two valves is such that one of them should
        before tripping off on low suction pressure. The most limiting accident
always remain in an open position to provide suction for emergency core
        requiring operation of the high pressure coolant injection system is a small
cooling through the high pressure coolant injection system.
        break loss-of-coolant accident and, for accident analysis purposes, high
The licensee concluded that, had the high pressure coolant injection system
        pressure coolant injection is considered inoperable. The response of the
been required, it would have functioned as designed for as long as 10 minutes
        plant to the small break loss-of-coolant accident has been predicted in~ the
before tripping off on low suction pressure.
        latest accident analysis.
The most limiting accident
        The licensee replaced the worn stem nut and reset the limit and torque switch
requiring operation of the high pressure coolant injection system is a small
        settings. The licensee established acceptance criteria for stem nut thread
break loss-of-coolant accident and, for accident analysis purposes, high
        inspection, but had not yet revised the maintenance procedure. The licensee
pressure coolant injection is considered inoperable.
        committed to provide detailed instructions for performing stem nut inspections
The response of the
        in the Limitorque maintenance procedures. Also, all_ Generic Letter 89-10
plant to the small break loss-of-coolant accident has been predicted in~ the
        safety-related motor-operated valves with rising stems which have original
latest accident analysis.
        stem nuts installed are being identified. Following the above activities, a
The licensee replaced the worn stem nut and reset the limit and torque switch
        representative sample of the motor-operated valves identified will have their
settings.
        stem nuts inspected to determine whether a potential motor-operated valve stem
The licensee established acceptance criteria for stem nut thread
        nut wear problem. exists.
inspection, but had not yet revised the maintenance procedure.
        The inspector reviewed the documentation of the completed corrective' actions
The licensee
        and concluded that the licensee's actions were appropriate.
committed to provide detailed instructions for performing stem nut inspections
        7.2   (closed) Licensee Event Report 298/92-012:     Inoperability of Reactor
in the Limitorque maintenance procedures. Also, all_ Generic Letter 89-10
              Core Isolation Coolina Motor-Operated-Valve Due to Water Intrusion into
safety-related motor-operated valves with rising stems which have original
              the Motor Operator
stem nuts installed are being identified.
        This_ event involved the surveillance testing on_the outboard _ steam supply
Following the above activities, a
        isolation valve to the reactor core isolation cooling system.     As part of the
representative sample of the motor-operated valves identified will have their
        surveillance, the outboard isolation valve was closed but failed to reopen
stem nuts inspected to determine whether a potential motor-operated valve stem
        when required. Upon investigation, moisture was discovered in the limit
nut wear problem. exists.
        switch box which caused the valve to not open. A hair-line crack was found in
The inspector reviewed the documentation of the completed corrective' actions
        the flexible conduit installed to protect the wiring between the limit switch
and concluded that the licensee's actions were appropriate.
                                                                                          -
7.2
(closed) Licensee Event Report 298/92-012:
Inoperability of Reactor
Core Isolation Coolina Motor-Operated-Valve Due to Water Intrusion into
the Motor Operator
This_ event involved the surveillance testing on_the outboard _ steam supply
isolation valve to the reactor core isolation cooling system.
As part of the
surveillance, the outboard isolation valve was closed but failed to reopen
when required. Upon investigation, moisture was discovered in the limit
switch box which caused the valve to not open. A hair-line crack was found in
the flexible conduit installed to protect the wiring between the limit switch
-


                                        .
.
    .
.
4
4
.
.
                                          -13-
-13-
  compartment and the terminal box. This crack was near a steam packing leak
compartment and the terminal box. This crack was near a steam packing leak
  which allowed moisture to enter the conduit line and travel into the limit
which allowed moisture to enter the conduit line and travel into the limit
  - switch box. The inboard and outboard isolation valves were both normally
- switch box. The inboard and outboard isolation valves were both normally
  open. The inboard isolation valve was operable.
open. The inboard isolation valve was operable.
  The licensee reduced power for ALARA purposes so that entry into the steam
The licensee reduced power for ALARA purposes so that entry into the steam
  tunnel for repair of the valve could be made safely. The corrective actions
tunnel for repair of the valve could be made safely.
                                                                  -
The corrective actions
  included drying out limit switch internals and replacing the valve motor
-
  degraded terminal blocks. A tee drain was installed n- the limit switch
included drying out limit switch internals and replacing the valve motor
  compartment cover to provide a drain path for any fF           moisture
degraded terminal blocks. A tee drain was installed n- the limit switch
  accumulation, and a shield was installed around the         .uit in the immediate
compartment cover to provide a drain path for any fF
  vicinity of the motor-operated valve. The licensee pians to replace the-
moisture
  cracked conduit during the 1993 refueling outage and to inspect other motor--
accumulation, and a shield was installed around the
  operated valve installations where flexible conduit containing motor-operator
.uit in the immediate
  leads may be in close proximity to valve packing glands.
vicinity of the motor-operated valve.
  The inspectors reviewed the documentation of the completion of the licensee's
The licensee pians to replace the-
  corrective actions and concluded that the licensee appropriately addressed
cracked conduit during the 1993 refueling outage and to inspect other motor--
  safety.
operated valve installations where flexible conduit containing motor-operator
  7.3   (Closed) Licensee Event Report 298/92-013:   Error in Limiting Single
leads may be in close proximity to valve packing glands.
        Failure Assumption for the Emergency Core Coolina System Performance
The inspectors reviewed the documentation of the completion of the licensee's
        Analysis
corrective actions and concluded that the licensee appropriately addressed
  This event involved the discovery of a nonconservativo assumption in the             '
safety.
  emergency core cooling system performance analysis, under postulated design
7.3
  basis loss-of-coolant accident conditions. The nonconservative assumption was
(Closed) Licensee Event Report 298/92-013:
  that the most limiting single failure was the_ failure-of one low pressure
Error in Limiting Single
  coolant injection subsystem injection valve. During the licensee's review of
Failure Assumption for the Emergency Core Coolina System Performance
  their design basis reconstitution program, they determined several failure
Analysis
  modes existed for the 125-Vdc power system which would result in a more
This event involved the discovery of a nonconservativo assumption in the
  limiting single failure condition than previously analyzed. The licensee's
emergency core cooling system performance analysis, under postulated design
  immediate corrective action was to. reduce power toward hot shutdown in 6 hours
'
  and cold shutdown in 30 hours as required by Technical Specifications,-and a
basis loss-of-coolant accident conditions. The nonconservative assumption was
  Notification of Unusual Event was declared. Prior to achieving hot shutdown,
that the most limiting single failure was the_ failure-of one low pressure
  a vendor analysis indicated that meeting the design basis for emergency core
coolant injection subsystem injection valve.
  cooling systems was possible with certain operating restrictions. An                 -
During the licensee's review of
  - operating restriction of 90 percent power was imposed and remained in effect.       ;
their design basis reconstitution program, they determined several failure
  until modifications were completed which restored the validity of the original
modes existed for the 125-Vdc power system which would result in a more
                                                                                        '
limiting single failure condition than previously analyzed. The licensee's
  assumptions-used in the emergency core cooling system performance loss-of-
immediate corrective action was to. reduce power toward hot shutdown in 6 hours
  coolant analysis.
and cold shutdown in 30 hours as required by Technical Specifications,-and a
  On September 14, 1992, the licensee completed Design Change 92-141B which
Notification of Unusual Event was declared.
  allowed control of low pressure coolant injection and -reactor recirculation
Prior to achieving hot shutdown,
  discharge valves to be independent of the 125-Vdc battery system and, thus,_
a vendor analysis indicated that meeting the design basis for emergency core
  not subject to failure due to loss of one 125-Vdc battery system.
cooling systems was possible with certain operating restrictions. An
  The inspector observed changes made to the 250-Vdc control power and verified
-
  documentation for completion of the design change.
- operating restriction of 90 percent power was imposed and remained in effect.
                                    _.   _                 __     _                 .
';
until modifications were completed which restored the validity of the original
assumptions-used in the emergency core cooling system performance loss-of-
coolant analysis.
On September 14, 1992, the licensee completed Design Change 92-141B which
allowed control of low pressure coolant injection and -reactor recirculation
discharge valves to be independent of the 125-Vdc battery system and, thus,_
not subject to failure due to loss of one 125-Vdc battery system.
The inspector observed changes made to the 250-Vdc control power and verified
documentation for completion of the design change.
_.
_
__
_
.


                      ._.
._.
                      .
.
    .
.
                                                            -14-
-14-
                      8 MANAGEMENT MEETINGS (30702)
8 MANAGEMENT MEETINGS (30702)
                      On September 25, 1992, the Region IV Regional Administrator and members of his
On September 25, 1992, the Region IV Regional Administrator and members of his
                      staff accompanied the resident inspectors on a site tour and attended a
staff accompanied the resident inspectors on a site tour and attended a
                      presentation by the licensee. The licensee presentation included site
presentation by the licensee.
                      communications, quality assurance training, and their deficiency reporting
The licensee presentation included site
                      program, followed by an open discussion between the licensee and the NRC
communications, quality assurance training, and their deficiency reporting
                      staff.
program, followed by an open discussion between the licensee and the NRC
                      On October 1 and 2, the Division Director for the Division of Reactor Projects
staff.
                      was onsite for a site tour and discussions with select members of the                       .-
On October 1 and 2, the Division Director for the Division of Reactor Projects
                      licensee's staff.
was onsite for a site tour and discussions with select members of the
.-
licensee's staff.
-
-
-
                                                                                                                    -
l
                                                                                                                      l
. . . . . . . . .
  . . . . . . . . . .
.
                              ..                                               ..         _ _ _ - - _ _ . _ - _ _
..
..
_ _ _ - - _ _ . _ - _ _


    . ..
.
                                                                                            ,
..
..
.,
,
                                        ATTACHMENT 1
..
                                                                          t
.,
      1 PERSONS CONTACTED
ATTACHMENT 1
      1.1   Li_censee Personnel
t
      R. L. Beilke, Radiological Support Manager                                         l
1 PERSONS CONTACTED
                                                                                          '
1.1
      L. E. Bray, Regulatory Compliance Specialist
Li_censee Personnel
      R. Brungardt, Operations Manager
R. L. Beilke, Radiological Support Manager
      M. A. Dean, Nuclear Licensing and Safety Supervisor
l
      J. W. Dutton, Nuclear Training Manager
L. E. Bray, Regulatory Compliance Specialist
      C. M. Estes, Senior Manager of Operations
'
      J. R. Flaherty, Engineering Manager
R. Brungardt, Operations Manager
      R. L. Gardner, Plant Manager
M. A. Dean, Nuclear Licensing and Safety Supervisor
      M. D. Hamm,_ Security Supervisor
J. W. Dutton, Nuclear Training Manager
      H. T. Hitch, Plant Services Manager
C. M. Estes, Senior Manager of Operations
      R. A. Jansky, Outage and Modifications Manager                                       -
J. R. Flaherty, Engineering Manager
      E. M. Mace, Senior Manager Site Support
R. L. Gardner, Plant Manager
      J. H.-Meacham, Site Manager
M. D. Hamm,_ Security Supervisor
      C. R. Moeller, Acting Technical Staff Manager
H. T. Hitch, Plant Services Manager
      S. M. Peterson, Senior Manager of Operations
R. A. Jansky, Outage and Modifications Manager
      G. E. Smith, Quality Assurance Manager
-
      M. E. Unruh, Maintenance Manager
E. M. Mace, Senior Manager Site Support
      R. L. Wenzl, NED Site Engineering Manager
J. H.-Meacham, Site Manager
      The personnel listed above attended the exit meeting held on November 16,
C. R. Moeller, Acting Technical Staff Manager
      -1992.   In addition to the personnel listed above,_the inspectors contacted
S. M. Peterson, Senior Manager of Operations
      other personnel during this inspection period.
G. E. Smith, Quality Assurance Manager
      2 EXIT MEETING
M. E. Unruh, Maintenance Manager
      An exit meeting was conducted on November 16, 1992.   During this meeting, the
R. L. Wenzl, NED Site Engineering Manager
      inspectors reviewed the scope and findings of this report. The. licensee did-
The personnel listed above attended the exit meeting held on November 16,
      not identify as proprietary any information provided to,_or reviewed by, the
-1992.
      inspectors.
In addition to the personnel listed above,_the inspectors contacted
                                                                                        .
other personnel during this inspection period.
                                                                                      K
2 EXIT MEETING
An exit meeting was conducted on November 16, 1992.
During this meeting, the
inspectors reviewed the scope and findings of this report.
The. licensee did-
not identify as proprietary any information provided to,_or reviewed by, the
inspectors.
.
K
}}
}}

Latest revision as of 20:11, 12 December 2024

Insp Rept 50-298/92-22 on 921004-1114.Violations Noted. Major Areas Inspected:Operational Safety Verification, Surveillance Observations & Licensee Event Repts
ML20126B852
Person / Time
Site: Cooper Entergy icon.png
Issue date: 12/14/1992
From: Gagliardo J
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION IV)
To:
Shared Package
ML20126B835 List:
References
50-298-92-22, NUDOCS 9212220245
Download: ML20126B852 (15)


See also: IR 05000298/1992022

Text

.-

,,

'

.

.

APPENDIX B

U.S. NUCLEAR REGULATORY COMMISSION

REGION IV

Inspection Report:

50-298/92-22

Operating License:

DPR-46

Licensee:

Nebraska Public Power District

P.O. Box 499

Columbus, Nebraska

68602-0499

Facility Name:

Cooper Nuclear Station

Inspection At:

Brownville, Nebraska

Inspection Conducted: October 4 through November 14, 1992

Inspectors:

R. A. Kopriva, Senior Resident Inspector

W. C. Walker, Resident Inspector

J. M. Keeton, Operator Licensing

Approv '

  1. o

yL

2. _['1

. Gagliardo,' liTeT7T jects section C

at

'

Inspection Summar_y

Areas Inspected:

Routine, unannounced inspection of onsite response to

events, operational safety verification, surveillance observations, followup,

and onsite review of licensee event reports.

Resulu:

Overall, the licensee operated the facility safety (paragraphs 2 and

e

3.5).

The licensee's evaluation and corrective actions to address the water

hammer event in Residual Heat Removal System B on October 22,-1992, were

prompt and appeared to be good (paragraph 2),

o

Housekeeping was improving.

Licensee management was addressing this

issue (paragraph 3.2).

A compressed gas cylinder was not properly controlled on the refueling -

e

floor for an extended period of time.

This is a violation

(paragraph 3.2),

One example of improper control of visitors was identified. This is a

e

violation (paragraph 3.4).

Surveillance tests were performed well.

The licensee personnel involved

were knowledgeable of the tasks required and their actions were good

(paragraph 4.3).

9212220245 921214

DR

ADOCK 05000298

PDR

,

_

_

.

_.

_.

.

..

.

+

-2-

The maintenance activity to repair and inspect the faulty diesel

generator fuse holders was good (paragraph 5.1).

The licensee appropriately addressed, from a safety perspective, the use

s

of a process can in the spent fuel pool (paragraph 6.3).

Licensed operator training weaknesses were observed in command, control,

and communications; however, the licensee was aware of the problems and

was actively pursuing their corrective actions program.

The simulator

evaluators were very professional and exhibited good evaluation skills.

Examination material was very good and in accordance with the standard.

The licenset operators appeared to be safety-conscious and competent

(paragraph 6.5).

Summar.y of Inspection Findings:

e

Violation 298/9222-01 was opened (paragraph 3.2).

e

Violation 298/9222-02 was opened (paragraph 3.4).

Inspection Followup Item 298/9034-02 was closed (paragraph 6.1).

e

Unresolved Item 298/9219-01 was closed (paragraph 6.2).

e

Unresolved Item 298/9219-02 was closed (paragraph 6.3).

Licensee Event Reports92-008, 92-012, and 92-013 were closed

(paragraph 7).

Attachments (and/or Enclosures):

e

Attachment 1 - Persons Contacted and Exit Meeting

. - - - .

_- _

-.

_

.. _ _._.

4

I

t

,

_3

DETAILS

1 PLANT STATUS

$

At the beginning of this inspection period, the plant was operating at

53 percent power and in single-loop operation. On October 1, 1992, Reactor

Recirculation Motor-Generator Set B had tripped due to a faulty resistor and

two faulty diodes.

The components were replaced and the motor-generator set

was restarted.

The unit returned to full power on October 5.

At the end of

this inspection, the plant was operating at 100 percent power.

2 ONSITE RESPONSE TO EVENT (93702)

.

Residual Heat Removal System B Inoperable

On October 22, 1992, Residual Heat Removal System B was declared inoperable

during performance of Surveillance Procedure 6.3.5.1, "RHR Test Mode

Surveillance Operation Quarterly Inservice Test," Revision 35.

During the surveillance, Residual Heat Removal Pump B was run, determined to

be acceptable, and shut down.

Pump D was then aligned according to the

procedure, which took approximately 5 minutes.

Upon the starting of Pump D, a

loud noise was heard.

The licensee investigated the source of the noise and

located a leak on the 958 foot elevation of the reactor building, at the

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flange for Pressure Maintenance System Check Valve 19. The check valve was

located in a 4-inch line which is part of the auxiliary ccndensate system,

which provides pressure maintena e o r the residual heat removal system.

Approximately 50 gallons of wat e had leaked out of the system into the

reactor building.

Licensee empsoyees bserved that the bonnet gasket on Check

Valve 19 was unseated.

They pr3ce h

to walk down the remainder of the

pressure maintenance system and (Qsm ed two pipe supports which had been

deformed from-the event and als seve al pipe hangers which were misaligned.

The licensee determined that the n.

<et faih re and pipe damage were caused by

a water hammer.

The licensee reviewed past water hammer events that have occurred in boiling

water reactors, conducted system walkdowns, and assov.ed the impact the water

hammer had on the residual heat removal system. The licensee repaired the

pipe supports that were damaged and the check valve which was found to be

I

leaking due to the ';ent.

The check valve was functionally -tested and found

to be satisfactory.

Documentation was provided which showed that the event

had not compromised the system pressure boundary integrity in its repaired

configuration.

The licensee determined that the event was caused by valving out the pressure

maintenance system when switching over from Pump B to Pump D during the

surveillance test.

A procedure change had been made which requires that the

pressure maintenance system remain in service during pump changeover.

The

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inspectors reviewed the licensee's corrective actions and found them

appropriate.

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Conclusions

The licensee's evaluation and corrective actions were prompt and appeared to

be good.

3 OPERATIONAL SAFETY VERIFICATION (71707)

3.1 Control Room Observations

The inspectors observed operational activities throughout this inspection

period to verify that proper control room staffing and control room

professionalism were maintained.

Control room shift supervisor log book, tag

out log book, and control room balance-of-plant log book entries were reviewed

to verify that appropriate entries were made. The licensee's control of these

activities was good.

3.2 Plant Tours

The inspectors toured various areas of the plant to verify that proper

housekeeping was being maintained.

Housekeeping was found to be improving,

but su4e areas remained where additional improvement was needed.

The

licensee's increased efforts for improving housekeeping were evident and

management was continuing to review this activity.

On October 5, the inspectors found an unsecured, wheeled fire extinguisher in

the reartor building on the 958-foot elevation and questioned the licensee as

to what effect a seismic event would have on the unsecured fire extinguisher.

Approximately 15 feet separated the fire extinguisher cart from Fuel Pool

Cooling Instrument Rack 25-16 containing essential equipment. The licensee

performed a seismic analysis to determine whether the subject fire

extinguisher could have interacted with essential equipment.

The analysis

concluded that it would be unlikei) that the extinguisher would topple during

a seismic event. However, if it did tip over, there was no essential

eauipmerit located where it could interact with the extinguisher.

As a conservative measure, the licensee secured the extinguisher.

In

addition, the licensee reviewed six other wheeled fire extinguisher locations

within the plant to determine possible interaction of those extinguisbers with

essential equipment.

The licensee concluded that no concerns existed with the

six other wheeled fire extinguishers. The inspectors reviewed the licensee's

actions and considered them to be appropriate.

On October 6,1992, during a walkdown of the reactor building, the inspector

identified a gas cylinder in the northwest quadrant of the refueling floor

j

which was roped to the two-wheel cart used for transporting the gas cylinder.

The gas cylinder was not secured to a fixed restraint, the cart was not a

wheeled cart of approved design for storage or use, and the wheels of the cart

were not blocked or locked. At the time of discovery the inspector could not

identify a use for the cylinder or the status of the cylinder (i.e., whether

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it was full or empty). Under certain conditions, the cylinder could become a

missile and damage equipment or personnel on the refueling floor or equipment

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in the fuel pool.

The licensee determined that the gas cylinder was helium and that it had been

used on April 11 to leak test the reactor pressure vessel . surveillance

specimen shipping cask in accordance with Special Procedure 92-022.

The

special procedure did not include specific precautions or instructions for-

handling, storage, or removal of the gas cylinder- The licensee removed the

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gas cylinder from the refueling floor.

The protective cap was in place on the

cylinder and it was partially, if not completely, depressurized.

Title 10 CFR Part 50, Appendix B, Criterion V, states that activities

affecting quality shall be prescribed by documented instruction,

3rocedures,

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or drawings of a type appropriate to the circumstances and shall

ae

accomplished in accordance with these instructions, procedures, or drawings.

Procedure 0.7, Revision 8, " Flammable, Combustible, and Chemical Material

Control," paragraph-8.3.2.2.0, states that, during storage and use, gas

cylinders shall be individually secured to a fixed suppor.t by a restraint, and

paragraph 8.3.2.3 states that use of wheel-mounted carts of approved design

are permitted for certain uses of gas cylinders. .The helium gas cylinder had

been on the refueling floor since approximately April 11 and on October 6 was

not secured to a fixed support and was not on a wheel-mounted cart of approved

design.

This is a violation.(298/9222-01).

3.3 Radiological Protection Observations

The inspectors verified that selected radiological protection activities were

in conformance with facility policies, procedures, and regulatory

requirements. Radiation and/or contaminated areas were properly posted and

controlled.

3.4 Security Program Observations

On October 5, the inspectors observed a repairman, with a visitor's badge, on

the_ first floor of the administration building, in a room with two separate

access points, and he was not within the line of sight of his escort.

One

access point would have allowed the repairman to leave the-work area-unseen by

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the escort and obtain access to other areas within the protected area. ..The-

inspectors asked the repairman about his escort. The repairman thought he

could identify his escort, but was uncertain where the escort was. The

inspectors located the escort. The escort had assumed that the access door

leading from the work room to other areas within the plant was closed. After

o

being questioned by the inspectors,=the door was closed.

However, there was

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no way to lock this door which would prevent the repairman from exiting

unobserved. The inspectors promptly reported the situation ~to station

security and a security officer was dispatched to review the situation.

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The inspectors reviewed the licensee's escort training and training

documentation.

The escort training lesson plan and Visitor / Tour Station

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Access Procedure 1.15 provided instructions to escorts to maintain positive

control of visitors.

The individual responsible for escorting the repairman

had received the training. The licensee counseled the individual responsible

for escorting the visitor to ensure understanding of proper escort procedures,

On October 5, Security Event Report 92-224 was completed, which outlined the

event details.

immediate corrective actions included providing an escort for

the repairman and sending a security guard to the incident location to review

the situation.

The licensee also counselled the individual, emphasizing

instructions regarding visitor control requirements. The licensee was

reviewing the procedures to determine their adequacy, and long-ierm corrective

actions had not been established at the end of this report period.

Title 10 CFR 50.34(c) requires that each application for a license to operate

a production or utilization facility shall include a physical security plan.

The Cooper Nuclear Station Physical Security Plan, Section 1.5.2, requires

that escorts exercise and maintain control of their visitors at all times.

Cooper- Nuclear Station Operations Manual, Plant Services Procedure 1.15,

,

" Visitor / Tour Station Access," Revision 8, Section 4.2.1, states that an

escort is responsible to exercise and maintain control of the visitor at all

times,

The failure to exercise and maintain control of a visitor (i.e., an

individual not authorized by the licensee to enter protected areas without an

escort) while the visitor was working within the protected area on October 5,

1992, is a violation of NRC requirements (298/9222-02).

3.5 Conclusions

Overall, the licensee operated the facility safely,

Housekeeping was improving.

Licensee management was addressing this

issue.

A compressed gas cylinder was not properly controlled on the refueling

floor for an extended period of time.

This is a violation.

One example _of- improper control of visitors was identified.

This is a

violation.

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SURVEILLANCE 0BSERVATIONS (61726)

4.1 Undervoltage Relays and Rela _y Timers Functional Test

On October 16, 1992, the inspector observed the performance of Surveillance-

Procedure 6.2.2.1.10. "4160V Buses If and 1G Undervoltage Relays and Relay

Timers Functional Test," Revision 18.

Operators appeared to be following the surveillance procedure both locally and

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in the control room.

Good communications were noted between the control room

operators and individuals performing the surveillance.

In reviewing the

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procedures the inspector noted that proper signatures and approvals were

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evident.

During the surveillance the inspector observed that the conditions

inside the 4160V breaker cabinets were clean.

4.2 Reactor Core isolation Coolina Steam line Hiah Flow Calibration and

Functional Test

On October 28 the inspectors observed performance of Surveillance

Procedure 6.2.2.6.1 " Reactor Core Isolation Cooling Steam Line High Flow

Calibration and Functional Test," Revision 21. The inspector observed an-

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instrument mechanic performing the calibration of the differential pressure

switches which are used to monitor reactor core isolation cooling steam line

fl ow. The instrument mechanic was adhering to the procedure and-m..intained

good communications with the control room operators-throughout the

surveillance.

The instrument mechanic was conscientious in complying with

good radiological practice as he routinely changed protective gloves during

his manipulation of the valves associated with the differential pressure

switches.

The surveillance was completed satisfactorily with no anomalies

encountered.

4.3 Conclusions

The surveillances observed were performed well.

The licensee personnel:

involved were knowledgeable of the tasks required and executed these tasks

sufficiently to comply with the procedures. The inspectors found the licensee

actions, as they pertained to these surveillances, to be good,

5 MAINTENANCE OBSERVATION (62703)

On November 10, 1992, during a routine surveillance run of Emergency Diesel

Generator 1, it was noted that.the air start solenoid to_one bank of air

cylinders had not actuated.

Upon'further investigation, the licensee found

the fuse holder for that solenoid to be loose.

The inspectors observed the corrective: maintenance activity to repair the fuse

holder and the panel inspections-to check other fuse holders that may have-

experienced similar problems. The licensee did not -identify any addition

examples.of this deficiency. The inspectors verified ~that the workers

obtained proper authorization to perform the work, _that control room operators

were cognizant.of the maintenance activity, that workers followed'the

maintenance instructions, and that appropriate safety. precautions were taken

for work in energized panels. The inspector observed the postmaintenance

functional check of the solenoid and verified proper operation.

The

inspectors noted that the electrical cabinets were clean.

No unacceptable-

conditions were identified.

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5.1 Conclusion

The maintenance activity to repair and inspect _ i -

>olders was good.

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6 FOLLOWUP (92701)

6.1

(Closed) Inspection Followup Item 298/9034-02:

Entry into a Technical

Specification Limittna Condition for Operation During the Performance of

Surveillance Testing

The resident inspectors reviewed a licensee memorandum dated April 17, 1991,

which outlined proposed technical guidance and reflected existing policy on

the subject of entering Technical Specification. action statements during the

performance of surveillance testing.

The licensee had identified several

cases where procedures could disable a safety function during the performance

of a routine test.

As a result, several procedures were revised.

Certain

Technical Specification surveillance requirements have been amended to change

the test frequency to allow the performance of the st/veillance procedures

during refueling shutdowns instead of performing these at power.- Also, a

Technical Specification amendment eliminated the testing of certain systems

and components following the failure of a redundant system or component, a

practice which could result in the removal from service of the only operable

system or component. The licensee has taken further action to address the

issue of operability during the performance of surveillance procedures by

organizing a task force to identify additional required changes in the

surveillance program and Technical Specifications.

6.2 _(Closed) Unresolved Item 298/9219-01:

Implementina Organizational Change

without Having Amended the Technical Specifications

The licensee implemented a site reorganization on July 20, 1992, and had not

revised their Technical Specifications to reflect the changes in the

reorganization.

On October 8, the licensee submitted their-Technical

Specification amendment to the Commission.

Inspectors reviewed, for the time

between reorganization and submittal of the amendment, the person assigned

full. time responsibility for the operation of the facility as specified in

Technical Specification 6.1.1.

The inspectors concluded that the licensee met

Technical Specification 6.1.1 during this time period.

6.3 LClosed) Unresolved item 298/9219-02:

Potential Failure to Perform a

10 CFR 50.59 Review for Eauipraent Placed on Ten of Empty Spent Fuel Racks

On September 25, 1992, during a plant walkdown, the inspector identified a

process can located on top of empty spent fuel racks.

The process can was

used as part of the licensee's spent fuel pool cleanup project.

The

inspectors questioned whether a 10 CFR 50.59-evaluation for the process can

pertaining to its location on the spent fuel racks had been performed.

The process can was 2 feet in diameter by 4 feet long with a fully loaded

weight of.approximately 800 pounds. An engineering evaluation had been

performed prior to placement of the can on the spent fuel racks, to ensure

that the racks would handle the fully loaded weight of the can.

Also, the

licensee considered the possibility of damaging fuel assemblies should a

seismic event or industrial accident happen.

Interaction between the can and

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spent fuel assemblies was not deemed to be credible _because of the 20-foot

distance between the can and the storage racks containing spent fuel.

The licensee concluded that the calculated design basis seismic force would

overcome the friction between the process can and the spent fuel rack before

tipping the can, therefore, the can would remain upright-and horizontal

movement would be limited because of the oscillating nature of a seismic

event.

lhe can was submerged in water which had a dampening effect on any

movement of the can.

If the process can were to slice or roll far enough to

impact fuel bundles, damage to the fuel assemblies would not be expected.

The

fuel manufacturer estimated that it would take 250 foot-pounds of downward

impact loading to damage one fuel rod.

further, the licensee's_ Refuel

Accident Radiological Effects Calculation (No, NEDC 88-171), which assumes

111 rods to be broken, concludes that the resulting lifetime-thyroid and whole

body dose would be less than 1 percent of the NRC 10 CFR Part 100 reactor

siting criteria. The relationship between a vertical drop loading and a side

loading (assuming the process can moves horizontally) would not be one to one.

The 800 pound process can would have to free-fall approximately 34 feet- to

damage 111 fuel rods.

This amount of energy would not be attainable for the

configuration and controls the licensee had in place for the process can.

If

the can were to move in a direction away from the spent fuel, it could

possibly fall into the cask pad area of the fuel pool.

This accident would be

significantly less severe than the shipping cask drop accident analyzed in

Burns & Roe Calculation 2520-02.

Concerns for loose parts-(i.e., if the can were to topple over) falling into

the spent fuel pool or even potentially being transported into the reactor

have been addressed in bounding analysis previously completed for the site.

The licensee concluded that, with the procedures being used, the location of

the process can in the spent fuel pool, and the previous analysis performed,

all safety questions / concerns pertaining to the process can had been

addressed.

The inspectors concluded that the licensee's evaluation of the use of the

process can was appropriate.

6.4 Licensed Operator Requalification Program Evaluation

?*

On November 4 and 5, 1992, the resident inspector and a Region-based inspector

observed some requalification examinations, interviewed on-shift' supervisors,

and reviewed training and testing material. . Also, the licensed operators were

observed during the simulator examinations to determine if they were

conducting activities in a manner conducive to protection of the public health

and safety.

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The following previously identified weaknesses (from NRC Inspection

Report 50-298/9102) were specifically addressed either by direct observation,

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interviews, or by reviewing training program records:

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Crew command, control, and communication

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Adequacy of simulator scenarios

Operators' ability to establish shutdown cooling

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Operators' ability to diagnose conditions

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Some communications weaknesses were seen during this inspection:

During one scenario, the supervisor directing panel activities was not

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concise in his directives. A lack of uniformity in communication among

crews was seen,

During another scenario, a supervisor directed an operator to establish

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torus spray.

The operator could not get torus spray started and did not

inform the supervisor, who assumed that the torus was being sprayed.

The communications problems observed were compensated by actions of the

operators such that safety problems did not develop and mitigation strategies

were not degraded. The facility managers stated that initiatives were in

progress to improve communications.

This was primarily being done in the

evaluation sessions during the requalification training.

There was no formal

classroom presentation geared to defining a communications policy.

Training Guide NTG 318, " Command and Control" and operations directive, "CNS

Communications," were developed to address command and control.

However,

there did not appear to be a formal method to define -their interrelationship.

Command and control training had been incorporated into the evaluation

sessions during requalification training, but there were no formal classroom

presentations scheduled to address this area.

A review of the training and testing material used for this requalification

cycle showed that the material was current-and that mechanisms were in place

to update the material.

The simulator scenarios developed for this. evaluation

were in accordance with the guidelines stated in NUREG-1021, " Operator-

L.icensing Examiner Standards," Revision 7.

Critical task identification and

task standard definitions were very good.

A review of the graded written-

examinations indicated that they were developed based on the sample-plan' and

that they discriminated at the proper level.

During the simulator scenarios and walkthroughs, conditions existed that

required establishing shutdown cooling.

The operators were able to perform

all operations necessary to ' accomplish shutdown cooling.

No errors were

noted.

The licensed operators observed during the simulator and walkthrough

examinations demonstrated the ability to diagnose events and conditions.

No.

errors were observed.

The facility evaluators conducted the dynamic simulator and walkthrough

examinations professionally and in accordance with the standards.

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evaluators were able to function autonomously without management interference

or visible constraints. During simulator evaluation sessions that were

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observed, the lead examiner elicited full participation from all evaluators.

Facility evaluations were consistent with their program guidance, and the

licensee took appropriate measures to preserve examination integrity.

Other observations made by the inspectors and connunicated to the licensee

include:

e

Shift technical advisor rotation policy and involvement during

requalification examinations was not fully understood by the shift

Crews.

Simulator difficultly with P-1 printout has contributed to negative

e

training.

Rather than following up when a P-1 was not obtained, the

crew assumed it was a simulator problem and simulated having a. printout.

At one point during a shift crew scenario, both reactor operators were

behind the control panels at the same time.

Based on inspectors' observations, the licensee has made progress to

e

increase operations' sense of ownership in training.

Areas of strength that were identified include:

Evaluators were very professional and exhibited good evaluation skills,

Examination material was very good and in accordance with the standard.-

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Licensed operators took a serious professional approach to the annual

evaluation.

Although weaknesses were seen in command, control, and communications, the

licensee was aware of the problems and was actively pursuing their corrective

actions program.

The licensed operators appeared to be' safety-conscious and

competent.

6.5 Conclusions

The licensee appropriately addressed, from a safety perspective, the use

e

of a process can in the spent fuel pool.

Licensed operator training weaknesses were observed in command, control,

and communications; however, the licensee was aware of the problems and

was actively pursuing their corrective actions program. The simulator

evaluators were very professional and exhibited good evaluation skills.

Examination material was very good and in accordance with the standard.

The licensed operators appeared to be safety-conscious and competent.

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7 ONSITE REVIEW 0F LICENSEE EVENT REPORTS (92700)

7.1

(Closed) Licensee Event Report 298/92-008:

Inoperability of the High

Pressure Coolant Injection System Due to Stem Nut Wear of a Motor-

Operated Valve

This licensee event report documented the licensee's determination that the

high pressure coolant injection valve, HPCI-MOV-58, which is the pump suction

valve from the torus, was not stroking properly.

During the running of

Surveillance Procedure 6.2.2.3.4, "HPCI Suppression Chamber and Emergency

Condensate Storage Tank Water Level Calibration and Functional / Functional Test

and Water Initiation," Revision 25, both HPCI-MOV-58 and HPCI-MOV-17,-the pump

suction valve from the emergency condensate storage tank, could have been

closed. The system logic for these two valves is such that one of them should

always remain in an open position to provide suction for emergency core

cooling through the high pressure coolant injection system.

The licensee concluded that, had the high pressure coolant injection system

been required, it would have functioned as designed for as long as 10 minutes

before tripping off on low suction pressure.

The most limiting accident

requiring operation of the high pressure coolant injection system is a small

break loss-of-coolant accident and, for accident analysis purposes, high

pressure coolant injection is considered inoperable.

The response of the

plant to the small break loss-of-coolant accident has been predicted in~ the

latest accident analysis.

The licensee replaced the worn stem nut and reset the limit and torque switch

settings.

The licensee established acceptance criteria for stem nut thread

inspection, but had not yet revised the maintenance procedure.

The licensee

committed to provide detailed instructions for performing stem nut inspections

in the Limitorque maintenance procedures. Also, all_ Generic Letter 89-10

safety-related motor-operated valves with rising stems which have original

stem nuts installed are being identified.

Following the above activities, a

representative sample of the motor-operated valves identified will have their

stem nuts inspected to determine whether a potential motor-operated valve stem

nut wear problem. exists.

The inspector reviewed the documentation of the completed corrective' actions

and concluded that the licensee's actions were appropriate.

7.2

(closed) Licensee Event Report 298/92-012:

Inoperability of Reactor

Core Isolation Coolina Motor-Operated-Valve Due to Water Intrusion into

the Motor Operator

This_ event involved the surveillance testing on_the outboard _ steam supply

isolation valve to the reactor core isolation cooling system.

As part of the

surveillance, the outboard isolation valve was closed but failed to reopen

when required. Upon investigation, moisture was discovered in the limit

switch box which caused the valve to not open. A hair-line crack was found in

the flexible conduit installed to protect the wiring between the limit switch

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compartment and the terminal box. This crack was near a steam packing leak

which allowed moisture to enter the conduit line and travel into the limit

- switch box. The inboard and outboard isolation valves were both normally

open. The inboard isolation valve was operable.

The licensee reduced power for ALARA purposes so that entry into the steam

tunnel for repair of the valve could be made safely.

The corrective actions

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included drying out limit switch internals and replacing the valve motor

degraded terminal blocks. A tee drain was installed n- the limit switch

compartment cover to provide a drain path for any fF

moisture

accumulation, and a shield was installed around the

.uit in the immediate

vicinity of the motor-operated valve.

The licensee pians to replace the-

cracked conduit during the 1993 refueling outage and to inspect other motor--

operated valve installations where flexible conduit containing motor-operator

leads may be in close proximity to valve packing glands.

The inspectors reviewed the documentation of the completion of the licensee's

corrective actions and concluded that the licensee appropriately addressed

safety.

7.3

(Closed) Licensee Event Report 298/92-013:

Error in Limiting Single

Failure Assumption for the Emergency Core Coolina System Performance

Analysis

This event involved the discovery of a nonconservativo assumption in the

emergency core cooling system performance analysis, under postulated design

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basis loss-of-coolant accident conditions. The nonconservative assumption was

that the most limiting single failure was the_ failure-of one low pressure

coolant injection subsystem injection valve.

During the licensee's review of

their design basis reconstitution program, they determined several failure

modes existed for the 125-Vdc power system which would result in a more

limiting single failure condition than previously analyzed. The licensee's

immediate corrective action was to. reduce power toward hot shutdown in 6 hours6.944444e-5 days <br />0.00167 hours <br />9.920635e-6 weeks <br />2.283e-6 months <br />

and cold shutdown in 30 hours3.472222e-4 days <br />0.00833 hours <br />4.960317e-5 weeks <br />1.1415e-5 months <br /> as required by Technical Specifications,-and a

Notification of Unusual Event was declared.

Prior to achieving hot shutdown,

a vendor analysis indicated that meeting the design basis for emergency core

cooling systems was possible with certain operating restrictions. An

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until modifications were completed which restored the validity of the original

assumptions-used in the emergency core cooling system performance loss-of-

coolant analysis.

On September 14, 1992, the licensee completed Design Change 92-141B which

allowed control of low pressure coolant injection and -reactor recirculation

discharge valves to be independent of the 125-Vdc battery system and, thus,_

not subject to failure due to loss of one 125-Vdc battery system.

The inspector observed changes made to the 250-Vdc control power and verified

documentation for completion of the design change.

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8 MANAGEMENT MEETINGS (30702)

On September 25, 1992, the Region IV Regional Administrator and members of his

staff accompanied the resident inspectors on a site tour and attended a

presentation by the licensee.

The licensee presentation included site

communications, quality assurance training, and their deficiency reporting

program, followed by an open discussion between the licensee and the NRC

staff.

On October 1 and 2, the Division Director for the Division of Reactor Projects

was onsite for a site tour and discussions with select members of the

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1 PERSONS CONTACTED

1.1

Li_censee Personnel

R. L. Beilke, Radiological Support Manager

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L. E. Bray, Regulatory Compliance Specialist

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R. Brungardt, Operations Manager

M. A. Dean, Nuclear Licensing and Safety Supervisor

J. W. Dutton, Nuclear Training Manager

C. M. Estes, Senior Manager of Operations

J. R. Flaherty, Engineering Manager

R. L. Gardner, Plant Manager

M. D. Hamm,_ Security Supervisor

H. T. Hitch, Plant Services Manager

R. A. Jansky, Outage and Modifications Manager

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E. M. Mace, Senior Manager Site Support

J. H.-Meacham, Site Manager

C. R. Moeller, Acting Technical Staff Manager

S. M. Peterson, Senior Manager of Operations

G. E. Smith, Quality Assurance Manager

M. E. Unruh, Maintenance Manager

R. L. Wenzl, NED Site Engineering Manager

The personnel listed above attended the exit meeting held on November 16,

-1992.

In addition to the personnel listed above,_the inspectors contacted

other personnel during this inspection period.

2 EXIT MEETING

An exit meeting was conducted on November 16, 1992.

During this meeting, the

inspectors reviewed the scope and findings of this report.

The. licensee did-

not identify as proprietary any information provided to,_or reviewed by, the

inspectors.

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