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{{#Wiki_filter:_ | {{#Wiki_filter:_.. | ||
VERMONT YANKEE | |||
. NUCLEIR POWER CORPORATION | |||
*MD. | |||
P.O. Box 157, Governor Hunt Road | |||
( %xy. | ( %xy. | ||
Yq 'N / ') | |||
d-' | W vernon, vermont 05354-0157 d-' | ||
/ | |||
(802) 257-7711 m. | |||
,s May 10,1994 VY-RCE-94-012 BVY 94-50 U.S. Nuclear Regulatory Commission Washington, D.C. 20555 Attn: | |||
Document Control Desk | |||
==Reference:== | ==Reference:== | ||
a) | a) | ||
License No. DPR-28 (Docket No. 50-271) | |||
==Dear Sir:== | ==Dear Sir:== | ||
Submitted herewith is the Monthly Statistical Report for the Vennont i | Submitted herewith is the Monthly Statistical Report for the Vennont i | ||
Yankee Nuclear Power Station for the month of April.1994. | Yankee Nuclear Power Station for the month of April.1994. | ||
Very truly yours, 2 | Very truly yours, 2 | ||
Vennont Yankee Nuclear Power Corp. | Vennont Yankee Nuclear Power Corp. | ||
N | N i. | ||
1-Donald A. Reid Vice President, Operations cc: | V-y 1-Donald A. Reid Vice President, Operations cc: | ||
USNRC, Region I USNRC Resident inspector, VYNPS | |||
.c 9405200290 940430 Y | |||
I PDR ADOCK 05000271 | |||
- l# | |||
W OUUUd | 'g ' | ||
.R PDR W OUUUd | |||
1 VERMONT YANKEE NUCLEAR POWER STATION MONTIIIJ STATISTICAL REPOl(T 94-04 FOlt TIIE MONTil OF APRIL 1994 DP 0411 Rev. 5 Page 1 ofI | |||
VERMONT YANKEE NUCLEAR POWER STATION MONTIIIJ STATISTICAL REPOl(T 94-04 FOlt TIIE MONTil OF APRIL 1994 DP 0411 Rev. 5 Page 1 ofI | |||
w | w OPERATING DATA REPORT F | ||
DOCKET NO 50-271 DATE 940510 COMPLETED BY G.A. WALLIN TELEPHONE (802)257-7711 OPERATTELETATHS 1. | |||
DOCKET | Unit Name: | ||
yfrmont YalDlLQ2 2. | |||
Reporting Period: | |||
April NOTES: | |||
: 3. Licensed Thermal Power (MWt):1593 | : 3. Licensed Thermal Power (MWt):1593 | ||
: 4. Nameplate Rating (Gross MWe) : 51Q 5. | |||
Design Electrical Rating (Net MWe) : | |||
: 6. Maximum Dependable Capacity (Gross MWe) : | 114 (oc) 504(cc) l | ||
7.-Maximum Dependable Capacity (Net MWe): | : 6. Maximum Dependable Capacity (Gross MWe) : | ||
111 7.-Maximum Dependable Capacity (Net MWe): | |||
1Q4 8. | |||
If changes, occur in capacity ratings (Items Number 3 through 7) since last report, give reasons: | |||
N/A t | N/A t | ||
9. | |||
: 10. Reasons for restrictions, if any: | Power level to which restricted, if any(Net MWe): | ||
N/A | |||
: 13. Reactor Reserve Shutdown Hours | : 10. Reasons for restrictions, if any: | ||
: 14. Hours Generator On-Line | N/A This Month Yr-to-Date Cumulative | ||
: 11. Hours in Reporting Period 719.00 2879.00 187703.00 a | |||
: 15. Unit Reserve Shutdown Hours | : 12. Number Of Hours Reactor was Critical 678.12 2838.12 154055.53 | ||
: 16. Gross Thermal Energy Generated (MWH) | : 13. Reactor Reserve Shutdown Hours 0.00 0.00 0.00 | ||
: 14. Hours Generator On-Line 667.82 2822 17 150937.79 | |||
: 19. Unit Service Factor | : 15. Unit Reserve Shutdown Hours 0.00 0.00 0.00 | ||
: 16. Gross Thermal Energy Generated (MWH) 1955857.00_ | |||
: 21. Unit Capacity Factor (Using MDC Net) | 4455498.00 225161169.50 17 Gross Electrical Energy Generated 357363.00 1509118.00 75028500.00 i | ||
: 22. Unit Capacity Factor (UJing DER Net) | : 18. Net Electrical Energy Generated (MWH) 343697.00 | ||
: 23. Unit Forced Outage Rate | _1451057.00 71298081.00 | ||
: 24. Shutdowns scheduled over next 6 months (Type, Date, and Duration of | : 19. Unit Service Factor 92.88 98.03 79 62 | ||
Each: | '2 0. Unit Availability Factor 92.88 98.03 79.69 | ||
: 21. Unit Capacity Factor (Using MDC Net) 94.85 100.00 74.69 | |||
: 22. Unit Capacity Factor (UJing DER Net) 133.00 98.06 73.23 | |||
: 23. Unit Forced Outage Rate 7.12 1.97-5.12 | |||
: 24. Shutdowns scheduled over next 6 months (Type, Date, and Duration of Each: | |||
N/A 4 | |||
: 25. If shut down at end of report period, estimated date of startup:N/A | : 25. If shut down at end of report period, estimated date of startup:N/A | ||
: 26. Units In Test Status (prior to commercial operation): N/A Forecast Achieved | : 26. Units In Test Status (prior to commercial operation): N/A Forecast Achieved | ||
INITIAL CRITICALITY | ,] | ||
INITIAL CRITICALITY INITIAL ELECTRICITY COMMERCIAL OPERATION VYDPF 0411.01 DP 0411 Rev. 5 Page 1 of 1 RT No. 13.F01.19F | |||
. ~. _ _.. | |||
_.m..m__.-.__ | |||
AVERAGE DAILY UNIT POWER LEVEL DOCKET NO. 50-'271 UNIT Vermont Yankee DATE 240510 COMPLETED BY G.A. | |||
DAY | WALLIN TELEPHONE | ||
_(802)257-7711 MONTH Apr,il__ | |||
l i | |||
DAY AVERAGE DAILY POWER LEVEL DAY AVERAGE DAILY POWER LEVEL I | |||
(MWe-Net) | |||
(MWe-Net) l 1. | |||
519 17, 520 2. | |||
519 18. | |||
520 | |||
*3. | |||
496 19. | |||
520 4. | |||
518 20. | |||
520 5. | |||
518 21. | |||
520 6. | |||
517 22. | |||
16, | 520 7. | ||
517 23. | |||
520 8. | |||
51.& | |||
24. | |||
519 9. | |||
518 25. | |||
520 10. | |||
29 26. | |||
519 11. | |||
0 27, 520 1 | |||
12. | |||
308 28. | |||
519 l | |||
13, 516 29. | |||
518 14, 518 30. | |||
519 15. | |||
520 31. | |||
16, 52.0 | |||
*23 hour day INSTRUCTIONS On this format, list the average daily unit power level in MWE-Net for each day in the reporting month. | |||
Compute to the nearest whole megawatt. | |||
VYDPF 0411.02 DP 0411 Rev. 5 Page 1 of 1 RT No. 13 F01.18V 1 | |||
.,,.. -. ~.. -.. _., _.. -,.. -.... _ _. _ _. _.. _. _.. -,. - - - | |||
,- I | |||
~ | |||
- l UNIT SHUTDOWNS AND POWER REDUCTIONS f | |||
REPORT MONTH APRIL DOCKET NO 50-271 UNIT NAME Vermont Yankee F | |||
DATE 940510 1 | DATE 940510 4 | ||
COMPLETED BY | 1 COMPLETED BY G.A. Wallin TELEPHONE (802)257-7711 1 | ||
2 3 | |||
4 No. | 4 5 | ||
4 No. | |||
Date Type Duration Reason Method of License System Component Cause and Corrective E | |||
94-04 940410 | (hours) | ||
i | Shutting Event Code Code Action to Prevent i | ||
Down Report # | |||
Recurrence Reactor 94-04 940410 F | |||
51.18 A | |||
3 94-04 HA VALVEX "C" moisuture separator high level. | |||
i Turbine tripped and j | |||
a reactor scram. | |||
I Replaced a faulty level cont]oller. | I Replaced a faulty level cont]oller. | ||
1 | } | ||
1 F: Forced 2 Reason: | |||
B-Maintenance or Test | 3 Method: | ||
E-Operator Training and l | 4 Exhibit G-Jnstructions S: Scheduled A-Equipment Failure (Explain) 1 - Manual for Preparacion of Data B-Maintenance or Test 2 - Manual Scram Entry Sheets for License j | ||
C-Refueling 3 - Automatic Scram Event Report (LER) File | |||
[ | |||
1 | D-Regulatory. Restriction 4 - Other (Explain) | ||
(NUREG 0161) | |||
E-Operator Training and l | |||
License Examination 5 Exhibit I - Same Source | |||
.VYDPF 0411.03 F-Administrative. | |||
DP 0411 Rev. 5 G-Operational Error (Explain) f Page 1 of 1 H-(Explain) j s | |||
i 1 | |||
,y- | |||
~ -. -. -.. | |||
DOCKET'NO. 50-271 | |||
.DATE 230510 d | |||
COMPLETED BY G.A. WALLIN TELEPHONE (802)257-7711 | |||
[ | [ | ||
REPORT MONTH April | |||
- SJJMMARY OF OPEBATING EXPEFJEE.CfES Highlighte Vermont Yankee operated at 92.2% of rated thermal power for the' month. | |||
' Gross electrical generation was 357.363 MWHe or 92.0% design electrical capacity. | |||
i Operating Summary i | i Operating Summary i | ||
-The following is a chronological description of plant operations including other pertinent items of interest for the month: | |||
At the beginning of the reporting period the plant was operating at 99.9% | |||
of rated thermal power. | of rated thermal power. | ||
940410 | 940410 At 0122 hours, turbine tripped and reactor scrammed, caused by a high level signal in the "C" moisture separator. | ||
high level signal in the "C" moisture separator. | (See Unit 4 | ||
a return to full power was initiated. | Shutdowns and Power Reductions) 940411 At 1815 hours, the reactor was critical following repairs; 940412 At 0433 hours, the turbine-generator was phased to the grid, and a return to full power was initiated. | ||
3 | |||
-f | -f | ||
.i i | |||
l 1 | l 1 | ||
i At the end of the reporting period the plant was operating at 99.9% of. | |||
rated thermal power. | rated thermal power. | ||
VYDPF 0411.-04 DP 0411 Rev. 5 | VYDPF 0411.-04 DP 0411 Rev. 5 | ||
Page 1 of 1 | ) | ||
Page 1 of 1 RT No. 13.F01.18X | |||
. ~ | |||
-}} | |||
Latest revision as of 09:12, 16 December 2024
| ML20070R608 | |
| Person / Time | |
|---|---|
| Site: | Vermont Yankee File:NorthStar Vermont Yankee icon.png |
| Issue date: | 04/30/1994 |
| From: | Reid D, Wallin G VERMONT YANKEE NUCLEAR POWER CORP. |
| To: | NRC OFFICE OF INFORMATION RESOURCES MANAGEMENT (IRM) |
| References | |
| BVY-94-50, VY-RCE-94-012, VY-RCE-94-12, NUDOCS 9405200290 | |
| Download: ML20070R608 (6) | |
Text
_..
VERMONT YANKEE
. NUCLEIR POWER CORPORATION
- MD.
P.O. Box 157, Governor Hunt Road
( %xy.
Yq 'N / ')
W vernon, vermont 05354-0157 d-'
/
(802) 257-7711 m.
,s May 10,1994 VY-RCE-94-012 BVY 94-50 U.S. Nuclear Regulatory Commission Washington, D.C. 20555 Attn:
Document Control Desk
Reference:
a)
License No. DPR-28 (Docket No. 50-271)
Dear Sir:
Submitted herewith is the Monthly Statistical Report for the Vennont i
Yankee Nuclear Power Station for the month of April.1994.
Very truly yours, 2
Vennont Yankee Nuclear Power Corp.
N i.
V-y 1-Donald A. Reid Vice President, Operations cc:
USNRC, Region I USNRC Resident inspector, VYNPS
.c 9405200290 940430 Y
I PDR ADOCK 05000271
- l#
'g '
.R PDR W OUUUd
1 VERMONT YANKEE NUCLEAR POWER STATION MONTIIIJ STATISTICAL REPOl(T 94-04 FOlt TIIE MONTil OF APRIL 1994 DP 0411 Rev. 5 Page 1 ofI
w OPERATING DATA REPORT F
DOCKET NO 50-271 DATE 940510 COMPLETED BY G.A. WALLIN TELEPHONE (802)257-7711 OPERATTELETATHS 1.
Unit Name:
yfrmont YalDlLQ2 2.
Reporting Period:
April NOTES:
- 3. Licensed Thermal Power (MWt):1593
- 4. Nameplate Rating (Gross MWe) : 51Q 5.
Design Electrical Rating (Net MWe) :
114 (oc) 504(cc) l
- 6. Maximum Dependable Capacity (Gross MWe) :
111 7.-Maximum Dependable Capacity (Net MWe):
1Q4 8.
If changes, occur in capacity ratings (Items Number 3 through 7) since last report, give reasons:
N/A t
9.
Power level to which restricted, if any(Net MWe):
N/A
- 10. Reasons for restrictions, if any:
N/A This Month Yr-to-Date Cumulative
- 11. Hours in Reporting Period 719.00 2879.00 187703.00 a
- 12. Number Of Hours Reactor was Critical 678.12 2838.12 154055.53
- 13. Reactor Reserve Shutdown Hours 0.00 0.00 0.00
- 14. Hours Generator On-Line 667.82 2822 17 150937.79
- 15. Unit Reserve Shutdown Hours 0.00 0.00 0.00
- 16. Gross Thermal Energy Generated (MWH) 1955857.00_
4455498.00 225161169.50 17 Gross Electrical Energy Generated 357363.00 1509118.00 75028500.00 i
- 18. Net Electrical Energy Generated (MWH) 343697.00
_1451057.00 71298081.00
- 19. Unit Service Factor 92.88 98.03 79 62
'2 0. Unit Availability Factor 92.88 98.03 79.69
- 21. Unit Capacity Factor (Using MDC Net) 94.85 100.00 74.69
- 22. Unit Capacity Factor (UJing DER Net) 133.00 98.06 73.23
- 23. Unit Forced Outage Rate 7.12 1.97-5.12
- 24. Shutdowns scheduled over next 6 months (Type, Date, and Duration of Each:
N/A 4
- 25. If shut down at end of report period, estimated date of startup:N/A
- 26. Units In Test Status (prior to commercial operation): N/A Forecast Achieved
,]
INITIAL CRITICALITY INITIAL ELECTRICITY COMMERCIAL OPERATION VYDPF 0411.01 DP 0411 Rev. 5 Page 1 of 1 RT No. 13.F01.19F
. ~. _ _..
_.m..m__.-.__
AVERAGE DAILY UNIT POWER LEVEL DOCKET NO. 50-'271 UNIT Vermont Yankee DATE 240510 COMPLETED BY G.A.
WALLIN TELEPHONE
_(802)257-7711 MONTH Apr,il__
l i
DAY AVERAGE DAILY POWER LEVEL DAY AVERAGE DAILY POWER LEVEL I
(MWe-Net)
(MWe-Net) l 1.
519 17, 520 2.
519 18.
520
- 3.
496 19.
520 4.
518 20.
520 5.
518 21.
520 6.
517 22.
520 7.
517 23.
520 8.
51.&
24.
519 9.
518 25.
520 10.
29 26.
519 11.
0 27, 520 1
12.
308 28.
519 l
13, 516 29.
518 14, 518 30.
519 15.
520 31.
16, 52.0
- 23 hour day INSTRUCTIONS On this format, list the average daily unit power level in MWE-Net for each day in the reporting month.
Compute to the nearest whole megawatt.
VYDPF 0411.02 DP 0411 Rev. 5 Page 1 of 1 RT No. 13 F01.18V 1
.,,.. -. ~.. -.. _., _.. -,.. -.... _ _. _ _. _.. _. _.. -,. - - -
,- I
~
- l UNIT SHUTDOWNS AND POWER REDUCTIONS f
REPORT MONTH APRIL DOCKET NO 50-271 UNIT NAME Vermont Yankee F
DATE 940510 4
1 COMPLETED BY G.A. Wallin TELEPHONE (802)257-7711 1
2 3
4 5
4 No.
Date Type Duration Reason Method of License System Component Cause and Corrective E
(hours)
Shutting Event Code Code Action to Prevent i
Down Report #
Recurrence Reactor 94-04 940410 F
51.18 A
3 94-04 HA VALVEX "C" moisuture separator high level.
i Turbine tripped and j
a reactor scram.
I Replaced a faulty level cont]oller.
}
1 F: Forced 2 Reason:
3 Method:
4 Exhibit G-Jnstructions S: Scheduled A-Equipment Failure (Explain) 1 - Manual for Preparacion of Data B-Maintenance or Test 2 - Manual Scram Entry Sheets for License j
C-Refueling 3 - Automatic Scram Event Report (LER) File
[
D-Regulatory. Restriction 4 - Other (Explain)
E-Operator Training and l
License Examination 5 Exhibit I - Same Source
.VYDPF 0411.03 F-Administrative.
DP 0411 Rev. 5 G-Operational Error (Explain) f Page 1 of 1 H-(Explain) j s
i 1
,y-
~ -. -. -..
DOCKET'NO. 50-271
.DATE 230510 d
COMPLETED BY G.A. WALLIN TELEPHONE (802)257-7711
[
REPORT MONTH April
- SJJMMARY OF OPEBATING EXPEFJEE.CfES Highlighte Vermont Yankee operated at 92.2% of rated thermal power for the' month.
' Gross electrical generation was 357.363 MWHe or 92.0% design electrical capacity.
i Operating Summary i
-The following is a chronological description of plant operations including other pertinent items of interest for the month:
At the beginning of the reporting period the plant was operating at 99.9%
of rated thermal power.
940410 At 0122 hours0.00141 days <br />0.0339 hours <br />2.017196e-4 weeks <br />4.6421e-5 months <br />, turbine tripped and reactor scrammed, caused by a high level signal in the "C" moisture separator.
(See Unit 4
Shutdowns and Power Reductions) 940411 At 1815 hours0.021 days <br />0.504 hours <br />0.003 weeks <br />6.906075e-4 months <br />, the reactor was critical following repairs; 940412 At 0433 hours0.00501 days <br />0.12 hours <br />7.159392e-4 weeks <br />1.647565e-4 months <br />, the turbine-generator was phased to the grid, and a return to full power was initiated.
3
-f
.i i
l 1
i At the end of the reporting period the plant was operating at 99.9% of.
rated thermal power.
VYDPF 0411.-04 DP 0411 Rev. 5
)
Page 1 of 1 RT No. 13.F01.18X
. ~
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