ML17306A626: Difference between revisions

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=Text=
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{{#Wiki_filter:ACCELERATED DISTjGBUTION DEMONSTPATION SYSTEM REGULA       Y   INFORMATION DISTRIBUTI       SYSTEM   (RIDS)
{{#Wiki_filter:ACCELERATED DISTjGBUTION DEMONSTPATION SYSTEM REGULA Y INFORMATION DISTRIBUTI SYSTEM (RIDS)
ACCESSION NBR:9204070050                 DOC.DATE:   92/03/25   NOTARIZED:   NO       DOCKET FACZL:STN-50-528 Palo Verde Nuclear Station,                 Unit 1, Arizona Publi 05000528 STN-50-529 Palo Verde Nuclear Station,                 Unit 2, Arizona Publi 05000529 STN-50-530 Palo Verde Nuclear Station,                 Unit 3, Arizona Publi 05000530 AUTH. NAME             AUTHOR AFFILIATION CONWAY,W.F.           Arizona Public Service Co.           (formerly Arizona Nuclear Power RECIP.NAME             RECIPIENT AFFILIATION MARTIN,J.B.             Region 5 (Post 820201)
ACCESSION NBR:9204070050 DOC.DATE: 92/03/25 NOTARIZED: NO DOCKET FACZL:STN-50-528 Palo Verde Nuclear Station, Unit 1, Arizona Publi 05000528 STN-50-529 Palo Verde Nuclear Station, Unit 2, Arizona Publi 05000529 STN-50-530 Palo Verde Nuclear Station, Unit 3, Arizona Publi 05000530 AUTH.NAME AUTHOR AFFILIATION CONWAY,W.F.
Arizona Public Service Co. (formerly Arizona Nuclear Power RECIP.NAME RECIPIENT AFFILIATION MARTIN,J.B.
Region 5 (Post 820201)


==SUBJECT:==
==SUBJECT:==
Discusses actions util has completed & those planned to address aspects of Salem Unit 2 turbine generator a fire event on 911109.
Discusses actions util has completed
DISTRIBUTION CODE: ZEOID COPIES RECEIVED:LTR TITLE: General (50 Dkt)-Insp Rept/Notice of Violation P         L  ENCL       SIZE:
& those planned to address aspects of Salem Unit 2 turbine generator a fire event on 911109.
DISTRIBUTION CODE:
ZEOID COPIES RECEIVED:LTR L ENCL P SIZE: 2 TITLE: General (50 Dkt)-Insp Rept/Notice of Violation Response NOTES:STANDARDIZED PLANT Standardized plant.
Standardized plant.
05000528 05000529 05000530 RECIPIENT ID CODE/NAME PD5 PD THOMPSON,M INTERNAL: ACRS
'EOD/DEIIB DEDRO
.NRR/DLPQ/LHFBPT NRR/DOEA/OEAB
'RR/DST/DIR 8E2 NUDOCS-ABSTRACT OGC/HDS1 RGN5 FILE 01 EXTERNAL: EG6G/BRYCEFJ.H.
NSIC COPIES LTTR ENCL RECIPIENT ZD CODE/NAME TRAMMELL,C AEOD AEOD/DSP/TPAB NRR MORISSEAU,D NRR/DLPQ/LPEB10 NRR/DREP/PEPB9H NRR/PMAS/ILRB12 OE DIR G
ILE 02 NRC PDR COPIES LTTR ENCL 1
1 1
1 1
1-1 1
NOTES:
NOTE TO ALL"RIDS" RECIPIENTS:
PLEASE HELP US TO REDUCE WAS'ONTACTTHE DOCUMENT CONTROL DESK, ROOM P 1-37 (EXT. 20079) TO ELIMINATEYOUR NAMEFROM DISTRIBUTION LISTS FOR DOCUMENTS YOU DON'T NEED!
TOTAL NUMBER OF COPIES REQUIRED:
LTTR 25 ENCL ~~ O


===Response===
Arizona Public Service Company P.O, BOX 53999
2 NOTES:STANDARDIZED PLANT                                                              05000528 Standardized plant.                                                           05000529 Standardized plant.                                                            05000530 RECIPIENT                COPIES            RECIPIENT          COPIES ID CODE/NAME              LTTR ENCL      ZD CODE/NAME        LTTR ENCL PD5 PD                                    TRAMMELL,C THOMPSON,M INTERNAL: ACRS                                          AEOD                    1
~
            'EOD/DEIIB                                  AEOD/DSP/TPAB            1 DEDRO                                    NRR MORISSEAU,D          1
PHOENIX. ARIZONA85072-3999 li~CC,l'.Ig lit"'.i R-"80HJ V l>>2 fi"h 27 I:ll [0: 26 WILLIAMF, CONWAY EXECUTIVEVICEPRESIDENT NUCLEAR 254-01969-WFC/8SE/RGK March 25, 1992 Mr. John B. Martin Regional Administration, Region V U.S. Nuclear Regulatory Commission 1450 Maria Lane, Suite 210 Walnut Creek, CA 94596-5368
            .NRR/DLPQ/LHFBPT                          NRR/DLPQ/LPEB10          1 NRR/DOEA/OEAB                            NRR/DREP/PEPB9H          1
          'RR/DST/DIR 8E2                              NRR/PMAS/ILRB12          1-NUDOCS-ABSTRACT                          OE DIR                  1 OGC/HDS1                                    G  ILE      02      1 RGN5    FILE    01 EXTERNAL: EG6G/BRYCEFJ.H.                              NRC PDR NSIC NOTES:
NOTE TO ALL "RIDS" RECIPIENTS:
PLEASE HELP US TO REDUCE WAS'ONTACT THE DOCUMENT CONTROL DESK, ROOM P 1-37 (EXT. 20079) TO ELIMINATEYOUR NAME FROM DISTRIBUTION LISTS FOR DOCUMENTS YOU DON'T NEED!
TOTAL NUMBER OF COPIES REQUIRED: LTTR                  25  ENCL    ~~    O
 
li~CC,l '.Ig lit"'.i R-"80HJ V Arizona Public Service Company P.O, BOX 53999 ~ PHOENIX. ARIZONA 85072-3999 l>>2 fi"h 27 I:ll [0: 26 WILLIAMF, CONWAY EXECUTIVEVICEPRESIDENT NUCLEAR 254-01969-WFC/8SE/RGK March 25, 1992 Mr. John B. Martin Regional Administration, Region V U.S. Nuclear Regulatory Commission 1450 Maria Lane, Suite 210 Walnut Creek, CA 94596-5368


==Reference:==
==Reference:==
Line 38: Line 50:


==Dear Mr. Martin:==
==Dear Mr. Martin:==
==Subject:==
==Subject:==
Palo Verde Nuclear Generating Station (PVNGS)
Palo Verde Nuclear Generating Station (PVNGS)
Line 44: Line 55:
Review of the November 9, 1991, Salem Unit 2 Turbine-Generator Overspeed and Fire Event File: 92-029-404 92-056-026 The purpose of this letter is to inform you of the actions Arizona Public Service Company (APS) has completed and those planned to address the aspects of the Salem Unit 2 Turbine-Generator and Fire Event.
Review of the November 9, 1991, Salem Unit 2 Turbine-Generator Overspeed and Fire Event File: 92-029-404 92-056-026 The purpose of this letter is to inform you of the actions Arizona Public Service Company (APS) has completed and those planned to address the aspects of the Salem Unit 2 Turbine-Generator and Fire Event.
On November 11, 1991, APS received notification over the Nuclear Network which
On November 11, 1991, APS received notification over the Nuclear Network which
        -included preliminary information concerning the Salem event. This information was distributed to management personnel at PVNGS via the PVNGS Tech News.
-included preliminary information concerning the Salem event.
In December 1991, PVNGS               formed a team to investigate this event for applicability to PVNGS. This investigation was based on the information available from the Nuclear Network; The details of NRC Information Notice 91-83 were included in the investigation
This information was distributed to management personnel at PVNGS via the PVNGS Tech News.
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In December 1991, PVNGS formed a team to investigate this event for applicability to PVNGS.
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This investigation was based on the information available from the Nuclear Network; The details of NRC Information Notice 91-83 were included in the investigation
                            'II2032
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$2040 0
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Mr. John B. Martin U.S.'Nuclear Regulatory Commission PVNGS Review of the NRC Region I AIT Report on the Salem Turbine-Generator Event Page 2 when APS received the Information Notice in late December. The investigative team considered system design and other factors that contributed to the Salem event. The three documents available from the Institute of Nuclear Power Operations and the Information Notice on this event were added to the. required reading list for the Operations Department. As an additional precaution, a pre-test briefing was conducted with all testing personnel prior to the January 9, 1992, overspeed test on Unit 2. Prior to this test, the investigative team reviewed the PVNGS Turbine-Generator System configuration and testing procedures to ensure that adequate controls were in place to avoid similar events at PVNGS.
Mr. John B. Martin U.S.'Nuclear Regulatory Commission PVNGS Review of the NRC Region I AIT Report on the Salem Turbine-Generator Event Page 2 when APS received the Information Notice in late December.
Upon receipt of the additional information included in the AIT report, the original review team (formed in December 1991) was expanded and charged with performing an in-depth review and application of lessons learned at PVNGS. The team is reviewing the event from a plant-wide perspective and will apply the lessons learned to the applicable plant systems, procedures, and programs. The PVNGS review team members have identified the areas of system design, system operation, system testing, system trending, operations procedures, preventative maintenance, emergency planning, and work control as the scope of their review. The preliminary review effort is complete, and the review team members are currently performing their in-depth reviews of assigned action area's.
The investigative team considered system design and other factors that contributed to the Salem event.
Corrective actions identified as a result of this review will be scheduled for implementation in a timely manner.
The three documents available from the Institute of Nuclear Power Operations and the Information Notice on this event were added to the. required reading list for the Operations Department.
As an additional precaution, a pre-test briefing was conducted with all testing personnel prior to the January 9, 1992, overspeed test on Unit 2.
Prior to this test, the investigative team reviewed the PVNGS Turbine-Generator System configuration and testing procedures to ensure that adequate controls were in place to avoid similar events at PVNGS.
Upon receipt of the additional information included in the AIT report, the original review team (formed in December 1991) was expanded and charged with performing an in-depth review and application of lessons learned at PVNGS. The team is reviewing the event from a plant-wide perspective and willapply the lessons learned to the applicable plant systems, procedures, and programs.
The PVNGS review team members have identified the areas of system design, system operation, system testing, system trending, operations procedures, preventative maintenance, emergency planning, and work control as the scope of their review.
The preliminary review effort is complete, and the review team members are currently performing their in-depth reviews of assigned action area's.
Corrective actions identified as a result of this review willbe scheduled for implementation in a timely manner.
If you have any questions, please contact Brad Ecklund of my staff at (602) 340-4068.
If you have any questions, please contact Brad Ecklund of my staff at (602) 340-4068.
Sincerely, j/     @ted<
Sincerely, j/
WFC/BSE/RGK/skk cc:   Document Control Desk D. H. Coe A: H. Gutterman A:,C. Gehr
@ted<
WFC/BSE/RGK/skk cc:
Document Control Desk D. H. Coe A: H. Gutterman A:,C. Gehr


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Latest revision as of 01:45, 8 January 2025

Discusses Actions Util Has Completed & Those Planned to Address Aspects of Salem Unit 2 Turbine Generator & Fire Event on 911109
ML17306A626
Person / Time
Site: Palo Verde  Arizona Public Service icon.png
Issue date: 03/25/1992
From: Conway W
ARIZONA PUBLIC SERVICE CO. (FORMERLY ARIZONA NUCLEAR
To: Martin J
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION V)
References
254-01969-WFC-B, 254-1969-WFC-B, NUDOCS 9204070050
Download: ML17306A626 (5)


Text

ACCELERATED DISTjGBUTION DEMONSTPATION SYSTEM REGULA Y INFORMATION DISTRIBUTI SYSTEM (RIDS)

ACCESSION NBR:9204070050 DOC.DATE: 92/03/25 NOTARIZED: NO DOCKET FACZL:STN-50-528 Palo Verde Nuclear Station, Unit 1, Arizona Publi 05000528 STN-50-529 Palo Verde Nuclear Station, Unit 2, Arizona Publi 05000529 STN-50-530 Palo Verde Nuclear Station, Unit 3, Arizona Publi 05000530 AUTH.NAME AUTHOR AFFILIATION CONWAY,W.F.

Arizona Public Service Co. (formerly Arizona Nuclear Power RECIP.NAME RECIPIENT AFFILIATION MARTIN,J.B.

Region 5 (Post 820201)

SUBJECT:

Discusses actions util has completed

& those planned to address aspects of Salem Unit 2 turbine generator a fire event on 911109.

DISTRIBUTION CODE:

ZEOID COPIES RECEIVED:LTR L ENCL P SIZE: 2 TITLE: General (50 Dkt)-Insp Rept/Notice of Violation Response NOTES:STANDARDIZED PLANT Standardized plant.

Standardized plant.

05000528 05000529 05000530 RECIPIENT ID CODE/NAME PD5 PD THOMPSON,M INTERNAL: ACRS

'EOD/DEIIB DEDRO

.NRR/DLPQ/LHFBPT NRR/DOEA/OEAB

'RR/DST/DIR 8E2 NUDOCS-ABSTRACT OGC/HDS1 RGN5 FILE 01 EXTERNAL: EG6G/BRYCEFJ.H.

NSIC COPIES LTTR ENCL RECIPIENT ZD CODE/NAME TRAMMELL,C AEOD AEOD/DSP/TPAB NRR MORISSEAU,D NRR/DLPQ/LPEB10 NRR/DREP/PEPB9H NRR/PMAS/ILRB12 OE DIR G

ILE 02 NRC PDR COPIES LTTR ENCL 1

1 1

1 1

1-1 1

NOTES:

NOTE TO ALL"RIDS" RECIPIENTS:

PLEASE HELP US TO REDUCE WAS'ONTACTTHE DOCUMENT CONTROL DESK, ROOM P 1-37 (EXT. 20079) TO ELIMINATEYOUR NAMEFROM DISTRIBUTION LISTS FOR DOCUMENTS YOU DON'T NEED!

TOTAL NUMBER OF COPIES REQUIRED:

LTTR 25 ENCL ~~ O

Arizona Public Service Company P.O, BOX 53999

~

PHOENIX. ARIZONA85072-3999 li~CC,l'.Ig lit"'.i R-"80HJ V l>>2 fi"h 27 I:ll [0: 26 WILLIAMF, CONWAY EXECUTIVEVICEPRESIDENT NUCLEAR 254-01969-WFC/8SE/RGK March 25, 1992 Mr. John B. Martin Regional Administration, Region V U.S. Nuclear Regulatory Commission 1450 Maria Lane, Suite 210 Walnut Creek, CA 94596-5368

Reference:

Letter dated January 24, 1992, from J. B. Martin, NRC, to.W. F. Conway, APS, "NRC Region I Augmented Inspection Team (AIT) Review of the November 9, 1991, Salem Unit 2 Turbine-Generator Overspeed and Fire Event"

Dear Mr. Martin:

Subject:

Palo Verde Nuclear Generating Station (PVNGS)

Units 1, 2, and 3 Docket Nos. STN 50-528/529/530 PVNGS Review of the NRC Region I Augmented Inspection Team (AIT)

Review of the November 9, 1991, Salem Unit 2 Turbine-Generator Overspeed and Fire Event File: 92-029-404 92-056-026 The purpose of this letter is to inform you of the actions Arizona Public Service Company (APS) has completed and those planned to address the aspects of the Salem Unit 2 Turbine-Generator and Fire Event.

On November 11, 1991, APS received notification over the Nuclear Network which

-included preliminary information concerning the Salem event.

This information was distributed to management personnel at PVNGS via the PVNGS Tech News.

In December 1991, PVNGS formed a team to investigate this event for applicability to PVNGS.

This investigation was based on the information available from the Nuclear Network; The details of NRC Information Notice 91-83 were included in the investigation

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( j I, I 4 '-." ~

$2040 0

g000528 050 'II2032 PDR S

I/O Md-og

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Mr. John B. Martin U.S.'Nuclear Regulatory Commission PVNGS Review of the NRC Region I AIT Report on the Salem Turbine-Generator Event Page 2 when APS received the Information Notice in late December.

The investigative team considered system design and other factors that contributed to the Salem event.

The three documents available from the Institute of Nuclear Power Operations and the Information Notice on this event were added to the. required reading list for the Operations Department.

As an additional precaution, a pre-test briefing was conducted with all testing personnel prior to the January 9, 1992, overspeed test on Unit 2.

Prior to this test, the investigative team reviewed the PVNGS Turbine-Generator System configuration and testing procedures to ensure that adequate controls were in place to avoid similar events at PVNGS.

Upon receipt of the additional information included in the AIT report, the original review team (formed in December 1991) was expanded and charged with performing an in-depth review and application of lessons learned at PVNGS. The team is reviewing the event from a plant-wide perspective and willapply the lessons learned to the applicable plant systems, procedures, and programs.

The PVNGS review team members have identified the areas of system design, system operation, system testing, system trending, operations procedures, preventative maintenance, emergency planning, and work control as the scope of their review.

The preliminary review effort is complete, and the review team members are currently performing their in-depth reviews of assigned action area's.

Corrective actions identified as a result of this review willbe scheduled for implementation in a timely manner.

If you have any questions, please contact Brad Ecklund of my staff at (602) 340-4068.

Sincerely, j/

@ted<

WFC/BSE/RGK/skk cc:

Document Control Desk D. H. Coe A: H. Gutterman A:,C. Gehr

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