PLA-0589, April 2005 Monthly Operating Reports for Susquehanna Steam Electric Station Units 1 and 2: Difference between revisions

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{{#Wiki_filter:% II Robert A.Saccone Vice President - Nuclear Operations PPL Susquehanna, LLC 769 Salem /Boulevard Berwick, PA 18603 Tel. 570.542.3959 Fax 570.542.1504 p % S I I l :--
{{#Wiki_filter:%
M RASaccone~pplweb.com May 10, 2005 U. S. Nuclear Regulatory Commission Attn: Document Control Desk Mail Stop O-PI-17 Washington, D.C. 20555-0001 SUSQUEHANNA STEAM ELECTRIC STATION MONTHLY OPERATING REPORTS Docket Nos. 50-387/NPF-14 and 50-388/NPF-22 PLA-05 898 The April 2005 Monthly Opeiating Reports for Susquehanua SES Units I and 2 are attached.
I I p l :--
% S I
I M
Robert A. Saccone Vice President - Nuclear Operations PPL Susquehanna, LLC 769 Salem /Boulevard Berwick, PA 18603 Tel. 570.542.3959 Fax 570.542.1504 RASaccone~pplweb.com May 10, 2005 U. S. Nuclear Regulatory Commission Attn: Document Control Desk Mail Stop O-PI-17 Washington, D.C. 20555-0001 SUSQUEHANNA STEAM ELECTRIC STATION MONTHLY OPERATING REPORTS Docket Nos. 50-387/NPF-14 and 50-388/NPF-22 PLA-05 898 The April 2005 Monthly Opeiating Reports for Susquehanua SES Units I and 2 are attached.
Very truly yours, JJH/cmm cc: NRC Region 1 NRC Sr. Resident Inspector, Mr. A. Blamey NRC Project Manager, Mr. R V. Guzman
Very truly yours, JJH/cmm cc: NRC Region 1 NRC Sr. Resident Inspector, Mr. A. Blamey NRC Project Manager, Mr. R V. Guzman


OPERATING DATA REPORT DOCKET NO. 50-387 UNIT        One DATE        05/10/2005 COMPLETED BY J. J. Hennings TELEPHONE    (570) 542-3747 OPERATING STATUS
OPERATING DATA REPORT DOCKET NO.
: 1. Unit Name:           Susquehanna Steam Electric Station (Ul)
UNIT DATE COMPLETED BY TELEPHONE 50-387 One 05/10/2005 J. J. Hennings (570) 542-3747 OPERATING STATUS
: 2. Reporting Period:             April 2005
: 1.
: 3. Design Electrical Rating (Net MWe): 1177
Unit Name:
: 4. Maximum Dependable Capacity (Net MWe):         1135 This Month  Yr.-to-Date  Cumulative
Susquehanna Steam Electric Station (Ul)
: 5. Hours in Reporting Period                                   719        2879.0    191,952.0
: 2.
: 6. Number of Hours Reactor Was Critical                         719        2879.0    160,867.0
Reporting Period:
: 7. Hours Generator On-Line                                     719        2879.0    158,479.0
April 2005
: 8. Unit Reserve Shutdown Hours                                   0            0            0
: 3.
: 9. Net Electrical Energy Generated (MWH)                     828,884     3,335,084   163,975,526 NOTES:
Design Electrical Rating (Net MWe):
1177
: 4.
Maximum Dependable Capacity (Net MWe):
1135
: 5.
Hours in Reporting Period
: 6.
Number of Hours Reactor Was Critical
: 7.
Hours Generator On-Line
: 8.
Unit Reserve Shutdown Hours
: 9.
Net Electrical Energy Generated (MWH)
This Month 719 719 719 0
828,884 Yr.-to-Date 2879.0 2879.0 2879.0 0
3,335,084 Cumulative 191,952.0 160,867.0 158,479.0 0
163,975,526 NOTES:
Page 1 of 1
Page 1 of 1


UNIT SHUTDOWNS DOCKET NO.             50-387 UNIT                    One DATE                    05/10/2005 COMPLETED BY            J. J. Hennings TELEPHONE              (570) 542-3747 REPORT MONTH April 2005 No.
UNIT SHUTDOWNS DOCKET NO.
Date Type     Duration         Reason     Method of                 Cause & Corrective Action (Hours)             2         Shutting                 To Prevent Recurrence Down
UNIT DATE COMPLETED BY TELEPHONE 50-387 One 05/10/2005 J. J. Hennings (570) 542-3747 REPORT MONTH April 2005 No.
_______
Date Type Duration Reason Method of Cause & Corrective Action (Hours) 2 Shutting To Prevent Recurrence Down R eactor3' No Reactor shutdowns this month Summary: There were no power reductions greater than 20% this month.
___  __ ___ ___    R eactor3' No Reactor shutdowns this month Summary: There were no power reductions greater than 20% this month.
1.
: 1.                                            2.                                            3.
F. Forced S. Scheduled 2.
F. Forced                                     Reason:                                        Method:
Reason:
S. Scheduled                                      A-   Equipment Failure (Explain)               1 - Manual B-   Maintenance or Test                       2 - Manual Scram C-   Refueling                                 3 - Automatic Scram D-   Regulatory Restriction                   4 - Continuation from previous month E - Operator Training & Licensee Exam         5 - Other F - Administrative G - Operational Error (Explain)
A - Equipment Failure (Explain)
Page 1 of I
B - Maintenance or Test C - Refueling D - Regulatory Restriction E - Operator Training & Licensee Exam F - Administrative G - Operational Error (Explain) 3.
Method:
1 - Manual 2 - Manual Scram 3 - Automatic Scram 4 - Continuation from previous month 5 - Other Page 1 of I


SUSQUEHANNA STEAM ELECTRIC STATION Docket Number: 50-387               Date: 05/10/05 Completed by: J. J. Hennings   Telephone: (570) 542-3747 Challenges to Main Steam Safety Relief Valves None.
SUSQUEHANNA STEAM ELECTRIC STATION Docket Number:
50-387 Completed by: J. J. Hennings Challenges to Main Steam Safety Relief Valves None.
Date:
05/10/05 Telephone:
(570) 542-3747


OPERATING DATA REPORT DOCKET NO. 50-388 UNIT        Two DATE        05/10/05 COMPLETED BY J. J. Hennings TELEPHONE    (570) 542-3747 OPERATING STATUS
OPERATING DATA REPORT DOCKET NO.
: 5. Unit Name:             Susquehanna Steam Electric Station (U2)
UNIT DATE COMPLETED BY TELEPHONE 50-388 Two 05/10/05 J. J. Hennings (570) 542-3747 OPERATING STATUS
: 6. Reporting Period:             April 2005
: 5.
: 7. Design Electrical Rating (Net MWe): 1182
Unit Name:
: 8. Maximum Dependable Capacity (Net MWe):         1140 This Month  Yr.-to-Date  Cumulative
Susquehanna Steam Electric Station (U2)
: 5. Hours in Reporting Period                                     719          2879      177,192
: 6. Reporting Period:
: 6. Number of Hours Reactor Was Critical                       626.66      2,198.6    154,878.4
April 2005
: 7. Hours Generator On-Line                                     597.13      2,128.2    152,820.9
: 7.
: 8. Unit Reserve Shutdown Hours                                   0            0          0
Design Electrical Rating (Net MWe):
: 9. Net Electrical Energy Generated (MWH)                     661,151     2,316,193   161,131,333 NOTES:
1182
Page 1 of I
: 8. Maximum Dependable Capacity (Net MWe):
1140
: 5.
Hours in Reporting Period
: 6.
Number of Hours Reactor Was Critical
: 7.
Hours Generator On-Line
: 8.
Unit Reserve Shutdown Hours
: 9.
Net Electrical Energy Generated (MWH)
NOTES:
This Month 719 626.66 597.13 0
661,151 Yr.-to-Date 2879 2,198.6 2,128.2 0
2,316,193 Cumulative 177,192 154,878.4 152,820.9 0
161,131,333 Page 1 of I


Ut UNIT SHUTDOWNS DOCKET NO.                 50-388 UNIT                        Two DATE                        05110105 COMPLETED BY                J. J. Hennings TELEPHONE                  (570) 542-3747 REPORT MONTH April 2005 No.       Date         Type         Duration         Reason     Method of                     Cause & Corrective Action (Hours)           2         Shutting                       to Prevent Recurrence Down Reactor 3
U t UNIT SHUTDOWNS DOCKET NO.
2     4/10/05         F           67.01             A             2         Manual scram due to loss of a 125V DC battery charger.
UNIT DATE COMPLETED BY TELEPHONE 50-388 Two 05110105 J. J. Hennings (570) 542-3747 REPORT MONTH April 2005 No.
Date Type Duration Reason Method of Cause & Corrective Action (Hours) 2 Shutting to Prevent Recurrence Down Reactor 3
2 4/10/05 F
67.01 A
2 Manual scram due to loss of a 125V DC battery charger.
The unit was returned to service on 4/13/05.
The unit was returned to service on 4/13/05.
3     4/28/05         F           54.86             A             2         Manual scram due to the loss of electrical supply to Main Transformer cooling. The unit was returned to service on 4130105.
3 4/28/05 F
54.86 A
2 Manual scram due to the loss of electrical supply to Main Transformer cooling. The unit was returned to service on 4130105.
Summary: Two manual shutdowns were required in April. The 4110/05 shutdown was required because a 125V DC battery charger failed and could not be repaired in the short time required by Susquehanna's Technical Specifications. The electrical component impacting the charger was replaced and the unit was returned to service on 4/13/05.
Summary: Two manual shutdowns were required in April. The 4110/05 shutdown was required because a 125V DC battery charger failed and could not be repaired in the short time required by Susquehanna's Technical Specifications. The electrical component impacting the charger was replaced and the unit was returned to service on 4/13/05.
The 4/28/05 shutdown was required to protect a main transformer from overheating due to the loss of the transformer cooling system electrical supply. An electrical short was repaired and the unit was returned to service on 4/30/05.
The 4/28/05 shutdown was required to protect a main transformer from overheating due to the loss of the transformer cooling system electrical supply. An electrical short was repaired and the unit was returned to service on 4/30/05.
: 1.                                                           2.                                                 3.
1.
F. Forced                                                     Reason:                                            Method:
2.
S. Scheduled                                                    A - Equipment Failure (Explain)                     I - Manual B - Maintenance or Test                           2 - Manual Scram C - Refueling                                       3 - Automatic Scram D - Regulatory Restriction                         4 - Continuation from previous month E - Operator Training & Licensee Exam               5 - Other F - Administrative G - Operational Error (Explain)
3.
Page 1 of 1
F. Forced S. Scheduled Reason:
A - Equipment Failure (Explain)
B - Maintenance or Test C - Refueling D - Regulatory Restriction E - Operator Training & Licensee Exam F - Administrative G - Operational Error (Explain)
Method:
I - Manual 2 - Manual Scram 3 - Automatic Scram 4 - Continuation from previous month 5 - Other Page 1 of 1


SUSQUEHANNA STEAM ELECTRIC STATION Docket Number:   50-388                 Date: 05/10/05 Completed by:   J. J. Hennings   Telephone: (570) 542-3747 Challenges to Main Steam Safety Relief Valves None.}}
SUSQUEHANNA STEAM ELECTRIC STATION Docket Number:
50-388 Date:
05/10/05 Completed by:
J. J. Hennings Telephone:
(570) 542-3747 Challenges to Main Steam Safety Relief Valves None.}}

Latest revision as of 18:38, 15 January 2025

April 2005 Monthly Operating Reports for Susquehanna Steam Electric Station Units 1 and 2
ML051440276
Person / Time
Site: Susquehanna  Talen Energy icon.png
Issue date: 05/10/2005
From: Saccone R
Susquehanna
To:
Document Control Desk, Office of Nuclear Reactor Regulation
References
PLA-05898
Download: ML051440276 (7)


Text

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% S I

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Robert A. Saccone Vice President - Nuclear Operations PPL Susquehanna, LLC 769 Salem /Boulevard Berwick, PA 18603 Tel. 570.542.3959 Fax 570.542.1504 RASaccone~pplweb.com May 10, 2005 U. S. Nuclear Regulatory Commission Attn: Document Control Desk Mail Stop O-PI-17 Washington, D.C. 20555-0001 SUSQUEHANNA STEAM ELECTRIC STATION MONTHLY OPERATING REPORTS Docket Nos. 50-387/NPF-14 and 50-388/NPF-22 PLA-05 898 The April 2005 Monthly Opeiating Reports for Susquehanua SES Units I and 2 are attached.

Very truly yours, JJH/cmm cc: NRC Region 1 NRC Sr. Resident Inspector, Mr. A. Blamey NRC Project Manager, Mr. R V. Guzman

OPERATING DATA REPORT DOCKET NO.

UNIT DATE COMPLETED BY TELEPHONE 50-387 One 05/10/2005 J. J. Hennings (570) 542-3747 OPERATING STATUS

1.

Unit Name:

Susquehanna Steam Electric Station (Ul)

2.

Reporting Period:

April 2005

3.

Design Electrical Rating (Net MWe):

1177

4.

Maximum Dependable Capacity (Net MWe):

1135

5.

Hours in Reporting Period

6.

Number of Hours Reactor Was Critical

7.

Hours Generator On-Line

8.

Unit Reserve Shutdown Hours

9.

Net Electrical Energy Generated (MWH)

This Month 719 719 719 0

828,884 Yr.-to-Date 2879.0 2879.0 2879.0 0

3,335,084 Cumulative 191,952.0 160,867.0 158,479.0 0

163,975,526 NOTES:

Page 1 of 1

UNIT SHUTDOWNS DOCKET NO.

UNIT DATE COMPLETED BY TELEPHONE 50-387 One 05/10/2005 J. J. Hennings (570) 542-3747 REPORT MONTH April 2005 No.

Date Type Duration Reason Method of Cause & Corrective Action (Hours) 2 Shutting To Prevent Recurrence Down R eactor3' No Reactor shutdowns this month Summary: There were no power reductions greater than 20% this month.

1.

F. Forced S. Scheduled 2.

Reason:

A - Equipment Failure (Explain)

B - Maintenance or Test C - Refueling D - Regulatory Restriction E - Operator Training & Licensee Exam F - Administrative G - Operational Error (Explain) 3.

Method:

1 - Manual 2 - Manual Scram 3 - Automatic Scram 4 - Continuation from previous month 5 - Other Page 1 of I

SUSQUEHANNA STEAM ELECTRIC STATION Docket Number:

50-387 Completed by: J. J. Hennings Challenges to Main Steam Safety Relief Valves None.

Date:

05/10/05 Telephone:

(570) 542-3747

OPERATING DATA REPORT DOCKET NO.

UNIT DATE COMPLETED BY TELEPHONE 50-388 Two 05/10/05 J. J. Hennings (570) 542-3747 OPERATING STATUS

5.

Unit Name:

Susquehanna Steam Electric Station (U2)

6. Reporting Period:

April 2005

7.

Design Electrical Rating (Net MWe):

1182

8. Maximum Dependable Capacity (Net MWe):

1140

5.

Hours in Reporting Period

6.

Number of Hours Reactor Was Critical

7.

Hours Generator On-Line

8.

Unit Reserve Shutdown Hours

9.

Net Electrical Energy Generated (MWH)

NOTES:

This Month 719 626.66 597.13 0

661,151 Yr.-to-Date 2879 2,198.6 2,128.2 0

2,316,193 Cumulative 177,192 154,878.4 152,820.9 0

161,131,333 Page 1 of I

U t UNIT SHUTDOWNS DOCKET NO.

UNIT DATE COMPLETED BY TELEPHONE 50-388 Two 05110105 J. J. Hennings (570) 542-3747 REPORT MONTH April 2005 No.

Date Type Duration Reason Method of Cause & Corrective Action (Hours) 2 Shutting to Prevent Recurrence Down Reactor 3

2 4/10/05 F

67.01 A

2 Manual scram due to loss of a 125V DC battery charger.

The unit was returned to service on 4/13/05.

3 4/28/05 F

54.86 A

2 Manual scram due to the loss of electrical supply to Main Transformer cooling. The unit was returned to service on 4130105.

Summary: Two manual shutdowns were required in April. The 4110/05 shutdown was required because a 125V DC battery charger failed and could not be repaired in the short time required by Susquehanna's Technical Specifications. The electrical component impacting the charger was replaced and the unit was returned to service on 4/13/05.

The 4/28/05 shutdown was required to protect a main transformer from overheating due to the loss of the transformer cooling system electrical supply. An electrical short was repaired and the unit was returned to service on 4/30/05.

1.

2.

3.

F. Forced S. Scheduled Reason:

A - Equipment Failure (Explain)

B - Maintenance or Test C - Refueling D - Regulatory Restriction E - Operator Training & Licensee Exam F - Administrative G - Operational Error (Explain)

Method:

I - Manual 2 - Manual Scram 3 - Automatic Scram 4 - Continuation from previous month 5 - Other Page 1 of 1

SUSQUEHANNA STEAM ELECTRIC STATION Docket Number:

50-388 Date:

05/10/05 Completed by:

J. J. Hennings Telephone:

(570) 542-3747 Challenges to Main Steam Safety Relief Valves None.