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{{#Wiki_filter: | {{#Wiki_filter:August 3, 2006 | ||
==SUBJECT:== | ==SUBJECT:== | ||
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Sincerely, | Sincerely, | ||
/RA/ | /RA/ | ||
Mark A. Ring, Chief Branch 1 Division of Reactor Projects Docket No. 50-461 License No. NPF-62 Enclosure: Inspection Report No. 05000461/2006004 w/Attachment: Supplemental Information cc w/encl: Site Vice President - Clinton Power Station Plant Manager - Clinton Power Station Regulatory Assurance Manager - Clinton Power Station Chief Operating Officer Senior Vice President - Nuclear Services Vice President - Operations Support Vice President - Licensing and Regulatory Affairs Manager Licensing - Clinton Power Station Senior Counsel, Nuclear, Mid-West Regional Operating Group Document Control Desk - Licensing Assistant Attorney General Illinois Emergency Management Agency State Liaison Officer, State of Illinois Chairman, Illinois Commerce Commission | Mark A. Ring, Chief Branch 1 Division of Reactor Projects Docket No. 50-461 License No. NPF-62 Enclosure: | ||
Inspection Report No. 05000461/2006004 w/Attachment: Supplemental Information cc w/encl: | |||
Site Vice President - Clinton Power Station Plant Manager - Clinton Power Station Regulatory Assurance Manager - Clinton Power Station Chief Operating Officer Senior Vice President - Nuclear Services Vice President - Operations Support Vice President - Licensing and Regulatory Affairs Manager Licensing - Clinton Power Station Senior Counsel, Nuclear, Mid-West Regional Operating Group Document Control Desk - Licensing Assistant Attorney General Illinois Emergency Management Agency State Liaison Officer, State of Illinois Chairman, Illinois Commerce Commission | |||
=SUMMARY OF FINDINGS= | =SUMMARY OF FINDINGS= | ||
| Line 48: | Line 50: | ||
===NRC-Identified and Self-Revealing Findings=== | ===NRC-Identified and Self-Revealing Findings=== | ||
===Cornerstone: Initiating Events=== | ===Cornerstone: Initiating Events=== | ||
* | |||
: '''Green.''' | : '''Green.''' | ||
On March 20, 2006, a finding of very low safety significance was self-revealed during an event. Clinton experienced a reactor scram due to a generator trip/lock out caused by an actuation of the generator differential overcurrent relay as a result of an open circuit on the C phase of the generator output current transformer. The open circuit was caused by burnt wires that resulted from inadequate workmanship, leaving terminal screws loose, following testing performed during the refueling outage in April 2002. The licensee checked all of the screws in the current transformer circuitry to ensure no others were loose, and implemented a temporary configuration change to remove the damaged phase from the circuitry. The licensee has scheduled replacement of the circuitry during the next refueling outage. | On March 20, 2006, a finding of very low safety significance was self-revealed during an event. Clinton experienced a reactor scram due to a generator trip/lock out caused by an actuation of the generator differential overcurrent relay as a result of an open circuit on the C phase of the generator output current transformer. The open circuit was caused by burnt wires that resulted from inadequate workmanship, leaving terminal screws loose, following testing performed during the refueling outage in April 2002. The licensee checked all of the screws in the current transformer circuitry to ensure no others were loose, and implemented a temporary configuration change to remove the damaged phase from the circuitry. The licensee has scheduled replacement of the circuitry during the next refueling outage. | ||
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===Licensee-Identified Violations=== | ===Licensee-Identified Violations=== | ||
No findings of significance were identified. | No findings of significance were identified. | ||
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===Summary of Plant Status=== | ===Summary of Plant Status=== | ||
The plant operated at approximately 96 percent rated thermal power (maintaining 104 percent electrical output) throughout the inspection period, with one brief reduction in power on May 21, 2006, to 79 percent, for a control rod sequence exchange. | The plant operated at approximately 96 percent rated thermal power (maintaining 104 percent electrical output) throughout the inspection period, with one brief reduction in power on May 21, 2006, to 79 percent, for a control rod sequence exchange. | ||
==REACTOR SAFETY== | ==REACTOR SAFETY== | ||
===Cornerstone: Initiating Events, Mitigating Systems, and Barrier Integrity=== | ===Cornerstone: Initiating Events, Mitigating Systems, and Barrier Integrity=== | ||
{{a|1R04}} | {{a|1R04}} | ||
==1R04 Equipment Alignment== | ==1R04 Equipment Alignment== | ||
{{IP sample|IP=IP 71111.04}} | {{IP sample|IP=IP 71111.04}} | ||
===.1 Partial Walkdowns=== | ===.1 Partial Walkdowns=== | ||
====a. Inspection Scope==== | ====a. Inspection Scope==== | ||
The inspectors performed partial walkdowns of accessible portions of divisions of risk-significant mitigating systems equipment during times when the divisions were of increased importance due to the redundant divisions or other related equipment being unavailable. The inspectors utilized the valve and electric breaker checklists listed in the to verify that the components were properly positioned and that support systems were lined up as needed. The inspectors also examined the material condition of the components and observed operating parameters of equipment to verify that there were no obvious deficiencies. The inspectors reviewed outstanding work orders and issue reports associated with the divisions to verify that those documents did not reveal issues that could affect division function. The inspectors used the information in the appropriate sections of the updated safety analysis report to determine the functional requirements of the systems. The documents listed at the end of this report were also used by the inspectors to evaluate this area. The inspectors performed four samples by verifying the alignment of the following divisions: | The inspectors performed partial walkdowns of accessible portions of divisions of risk-significant mitigating systems equipment during times when the divisions were of increased importance due to the redundant divisions or other related equipment being unavailable. The inspectors utilized the valve and electric breaker checklists listed in the to verify that the components were properly positioned and that support systems were lined up as needed. The inspectors also examined the material condition of the components and observed operating parameters of equipment to verify that there were no obvious deficiencies. The inspectors reviewed outstanding work orders and issue reports associated with the divisions to verify that those documents did not reveal issues that could affect division function. The inspectors used the information in the appropriate sections of the updated safety analysis report to determine the functional requirements of the systems. The documents listed at the end of this report were also used by the inspectors to evaluate this area. The inspectors performed four samples by verifying the alignment of the following divisions: | ||
| Line 84: | Line 84: | ||
===.2 Complete Walkdown=== | ===.2 Complete Walkdown=== | ||
====a. Inspection Scope==== | ====a. Inspection Scope==== | ||
The inspectors conducted a complete system alignment inspection of the reactor core isolation cooling system. This system was selected based on its high risk significance and mitigating systems function. The inspectors reviewed plant procedures, drawings, and the updated safety analysis report to identify proper system alignment and visually inspected system valves, instrumentation, and electrical supplies to verify proper alignment, component accessibility, availability, and current material condition. The inspectors also completed a review of corrective action documents, work orders, and operator work around and challenges to ensure there were no current operability concerns with the system. Documents reviewed during this inspection are listed in the | The inspectors conducted a complete system alignment inspection of the reactor core isolation cooling system. This system was selected based on its high risk significance and mitigating systems function. The inspectors reviewed plant procedures, drawings, and the updated safety analysis report to identify proper system alignment and visually inspected system valves, instrumentation, and electrical supplies to verify proper alignment, component accessibility, availability, and current material condition. The inspectors also completed a review of corrective action documents, work orders, and operator work around and challenges to ensure there were no current operability concerns with the system. Documents reviewed during this inspection are listed in the | ||
| Line 90: | Line 89: | ||
====b. Findings==== | ====b. Findings==== | ||
No findings of significance were identified. | No findings of significance were identified. {{a|1R05}} | ||
{{a|1R05}} | |||
==1R05 Fire Protection== | ==1R05 Fire Protection== | ||
{{IP sample|IP=IP 71111.05Q}} | {{IP sample|IP=IP 71111.05Q}} | ||
| Line 110: | Line 109: | ||
====b. Findings==== | ====b. Findings==== | ||
No findings of significance were identified. | No findings of significance were identified. {{a|1R06}} | ||
{{a|1R06}} | |||
==1R06 Flood Protection Measures== | ==1R06 Flood Protection Measures== | ||
{{IP sample|IP=IP 71111.06}} | {{IP sample|IP=IP 71111.06}} | ||
===.1 Internal Flooding=== | ===.1 Internal Flooding=== | ||
====a. Inspection Scope==== | ====a. Inspection Scope==== | ||
The inspectors verified that flooding mitigation plans and equipment were consistent with the design requirements and risk analysis assumptions. The inspectors reviewed the updated safety analysis report section 3.4.1 for internal flooding events and reviewed condition reports and work orders to complete one inspection sample on the following: | The inspectors verified that flooding mitigation plans and equipment were consistent with the design requirements and risk analysis assumptions. The inspectors reviewed the updated safety analysis report section 3.4.1 for internal flooding events and reviewed condition reports and work orders to complete one inspection sample on the following: | ||
| Line 121: | Line 120: | ||
====b. Findings==== | ====b. Findings==== | ||
No findings of significance were identified. | No findings of significance were identified. {{a|1R11}} | ||
{{a|1R11}} | |||
==1R11 Licensed Operator Requalification Program== | ==1R11 Licensed Operator Requalification Program== | ||
{{IP sample|IP=IP 71111.11}} | {{IP sample|IP=IP 71111.11}} | ||
===.1 Resident Inspector Quarterly Review=== | ===.1 Resident Inspector Quarterly Review=== | ||
====a. Inspection Scope==== | ====a. Inspection Scope==== | ||
The inspectors reviewed licensed-operator requalification training to evaluate operator performance in mitigating the consequences of a simulated event, particularly in the areas of human performance. The inspectors evaluated operator performance attributes which included communication clarity and formality, timely performance of appropriate operator actions, appropriate alarm response, proper procedure use and adherence, and senior reactor operator oversight and command and control. | The inspectors reviewed licensed-operator requalification training to evaluate operator performance in mitigating the consequences of a simulated event, particularly in the areas of human performance. The inspectors evaluated operator performance attributes which included communication clarity and formality, timely performance of appropriate operator actions, appropriate alarm response, proper procedure use and adherence, and senior reactor operator oversight and command and control. | ||
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====b. Findings==== | ====b. Findings==== | ||
No findings of significance were identified. | No findings of significance were identified. {{a|1R12}} | ||
{{a|1R12}} | |||
==1R12 Maintenance Effectiveness== | ==1R12 Maintenance Effectiveness== | ||
{{IP sample|IP=IP 71111.12Q}} | {{IP sample|IP=IP 71111.12Q}} | ||
| Line 153: | Line 152: | ||
====b. Findings==== | ====b. Findings==== | ||
No findings of significance were identified. | No findings of significance were identified. {{a|1R13}} | ||
{{a|1R13}} | |||
==1R13 Maintenance Risk Assessments and Emergent Work Control== | ==1R13 Maintenance Risk Assessments and Emergent Work Control== | ||
{{IP sample|IP=IP 71111.13}} | {{IP sample|IP=IP 71111.13}} | ||
| Line 169: | Line 168: | ||
====b. Findings==== | ====b. Findings==== | ||
No findings of significance were identified. | No findings of significance were identified. {{a|1R15}} | ||
{{a|1R15}} | |||
==1R15 Operability Evaluations== | ==1R15 Operability Evaluations== | ||
{{IP sample|IP=IP 71111.15}} | {{IP sample|IP=IP 71111.15}} | ||
| Line 179: | Line 178: | ||
* Operability assessment contained in issue report 487662, safety system annunciator power supply 1H13-P630 degraded; | * Operability assessment contained in issue report 487662, safety system annunciator power supply 1H13-P630 degraded; | ||
* Disposition of three NRC identified issues related to high pressure core spray; issue report 483115, seal wire separated for relief valve 1E22-F035, and issue report 487297, high pressure core spray acceptance criteria; | * Disposition of three NRC identified issues related to high pressure core spray; issue report 483115, seal wire separated for relief valve 1E22-F035, and issue report 487297, high pressure core spray acceptance criteria; | ||
* Licensees issue reports to assess the operability of the drywell floor drain system. Issue reports included: 496091, 1RF04T Hi-Hi Level alarm comes in before 1RF04PA starts; 482772, CPS 9543.09 Failed to work as written; and 484621, Incorrect counter number recorded during the performance of CPS 9543.10, Drywell Floor Drain Sump Level (1E31- N764) Channel Functional Test; | * Licensees issue reports to assess the operability of the drywell floor drain system. Issue reports included: 496091, 1RF04T Hi-Hi Level alarm comes in before 1RF04PA starts; 482772, CPS 9543.09 Failed to work as written; and 484621, Incorrect counter number recorded during the performance of CPS 9543.10, Drywell Floor Drain Sump Level (1E31-N764) Channel Functional Test; | ||
* Operability evaluation 472259-02 for reactor water level setpoint calculations cause inaccurate automatic trip module settings; | * Operability evaluation 472259-02 for reactor water level setpoint calculations cause inaccurate automatic trip module settings; | ||
* Operability evaluation 491911 for divisions 1 and 3 essential switchgear cooling unit, wrong code classification for condensing unit drain piping; and | * Operability evaluation 491911 for divisions 1 and 3 essential switchgear cooling unit, wrong code classification for condensing unit drain piping; and | ||
| Line 185: | Line 184: | ||
====b. Findings==== | ====b. Findings==== | ||
No findings of significance were identified. | No findings of significance were identified. {{a|1R19}} | ||
{{a|1R19}} | |||
==1R19 Post Maintenance Testing== | ==1R19 Post Maintenance Testing== | ||
{{IP sample|IP=IP 71111.19}} | {{IP sample|IP=IP 71111.19}} | ||
| Line 199: | Line 198: | ||
====b. Findings==== | ====b. Findings==== | ||
No findings of significance were identified. | No findings of significance were identified. {{a|1R22}} | ||
{{a|1R22}} | |||
==1R22 Surveillance Testing== | ==1R22 Surveillance Testing== | ||
{{IP sample|IP=IP 71111.22}} | {{IP sample|IP=IP 71111.22}} | ||
| Line 223: | Line 222: | ||
===Cornerstone: Emergency Preparedness=== | ===Cornerstone: Emergency Preparedness=== | ||
{{a|1EP6}} | {{a|1EP6}} | ||
==1EP6 Drill Evaluation== | ==1EP6 Drill Evaluation== | ||
{{IP sample|IP=IP 71114.06}} | {{IP sample|IP=IP 71114.06}} | ||
| Line 235: | Line 235: | ||
==OTHER ACTIVITIES== | ==OTHER ACTIVITIES== | ||
{{a|4OA1}} | {{a|4OA1}} | ||
==4OA1 Performance Indicator Verification== | ==4OA1 Performance Indicator Verification== | ||
{{IP sample|IP=IP 71151}} | {{IP sample|IP=IP 71151}} | ||
===Cornerstone: Initiating Events=== | ===Cornerstone: Initiating Events=== | ||
====a. Inspection Scope==== | ====a. Inspection Scope==== | ||
The inspectors sampled the licensees submittals for performance indicators for the period of April 2004 through March 2006. The inspectors used performance indicator definitions and guidance contained in revision 4 of Nuclear Energy Institute (NEI)document 99-02, Regulatory Assessment Performance Indicator Guideline to verify the accuracy of the performance indicator data. The inspectors performed three samples by reviewing the following: | The inspectors sampled the licensees submittals for performance indicators for the period of April 2004 through March 2006. The inspectors used performance indicator definitions and guidance contained in revision 4 of Nuclear Energy Institute (NEI)document 99-02, Regulatory Assessment Performance Indicator Guideline to verify the accuracy of the performance indicator data. The inspectors performed three samples by reviewing the following: | ||
| Line 246: | Line 247: | ||
====b. Findings==== | ====b. Findings==== | ||
No findings of significance were identified. | No findings of significance were identified. {{a|4OA2}} | ||
{{a|4OA2}} | |||
==4OA2 Identification and Resolution of Problems== | ==4OA2 Identification and Resolution of Problems== | ||
{{IP sample|IP=IP 71152}} | {{IP sample|IP=IP 71152}} | ||
| Line 255: | Line 256: | ||
====b. Findings==== | ====b. Findings==== | ||
No findings of significance were identified. | No findings of significance were identified. {{a|4OA3}} | ||
{{a|4OA3}} | |||
==4OA3 Event Follow-up== | ==4OA3 Event Follow-up== | ||
{{IP sample|IP=IP 71153}} | {{IP sample|IP=IP 71153}} | ||
causes turbine/generator trip and reactor scram. | ===.1 (Closed) Licensee Event Report 05000461/2006-01:=== | ||
Failure to tighten terminal screw causes turbine/generator trip and reactor scram. | |||
====a. Inspection Scope==== | ====a. Inspection Scope==== | ||
| Line 267: | Line 268: | ||
====b. Findings==== | ====b. Findings==== | ||
=====Introduction:===== | =====Introduction:===== | ||
A self-revealed Green finding was identified when a loose terminal screw on the C phase neutral current transformer of the main generator output caused the generator differential overcurrent 87-G1 relay to trip due to a sensed current imbalance resulting in a turbine/generator trip and reactor scram. | A self-revealed Green finding was identified when a loose terminal screw on the C phase neutral current transformer of the main generator output caused the generator differential overcurrent 87-G1 relay to trip due to a sensed current imbalance resulting in a turbine/generator trip and reactor scram. | ||
| Line 285: | Line 285: | ||
{{a|4OA6}} | {{a|4OA6}} | ||
==4OA6 Meetings== | ==4OA6 Meetings== | ||
===.1 Exit Meeting=== | ===.1 Exit Meeting=== | ||
The inspectors presented the inspection results to Mr. B. Hanson and other members of licensee management at the conclusion of the inspection on July 13, 2006. The inspectors asked the licensee whether any materials examined during the inspection should be considered proprietary. No proprietary information was identified. | The inspectors presented the inspection results to Mr. B. Hanson and other members of licensee management at the conclusion of the inspection on July 13, 2006. The inspectors asked the licensee whether any materials examined during the inspection should be considered proprietary. No proprietary information was identified. | ||
| Line 296: | Line 295: | ||
==KEY POINTS OF CONTACT== | ==KEY POINTS OF CONTACT== | ||
===Licensee personnel=== | ===Licensee personnel=== | ||
: [[contact::B. Hanson]], Site Vice President | : [[contact::B. Hanson]], Site Vice President | ||
| Line 316: | Line 314: | ||
==LIST OF ITEMS== | ==LIST OF ITEMS== | ||
===OPENED, CLOSED AND DISCUSSED=== | ===OPENED, CLOSED AND DISCUSSED=== | ||
===Opened and Closed=== | ===Opened and Closed=== | ||
: 05000461/2006004-01 | : 05000461/2006004-01 FIN Failure to tighten terminal screw causes turbine/generator trip and reactor scram due to inadequate workmanship. | ||
: 05000461/2006-01 | : 05000461/2006-01 LER Failure to tighten terminal screw causes turbine/generator trip and reactor scram. | ||
===Discussed=== | ===Discussed=== | ||
None. | None. | ||
==LIST OF DOCUMENTS REVIEWED== | ==LIST OF DOCUMENTS REVIEWED== | ||
}} | }} | ||
Latest revision as of 07:37, 15 January 2025
| ML062150271 | |
| Person / Time | |
|---|---|
| Site: | Clinton |
| Issue date: | 08/03/2006 |
| From: | Ring M NRC/RGN-III/DRP/RPB1 |
| To: | Crane C Exelon Generation Co, Exelon Nuclear |
| References | |
| IR-06-004 | |
| Download: ML062150271 (21) | |
Text
August 3, 2006
SUBJECT:
CLINTON POWER STATION - NRC INTEGRATED INSPECTION REPORT 05000461/2006004
Dear Mr. Crane:
On June 30, 2006, the U.S. Nuclear Regulatory Commission (NRC) completed an inspection at your Clinton Power Station. The enclosed inspection report documents the inspection results, which were discussed on July 13, 2006, with Mr. B. Hanson and other members of your staff.
This inspection examined activities conducted under your license as they relate to safety and compliance with the Commissions rules and regulations and with the conditions of your license.
The inspectors reviewed selected procedures and records, observed activities, and interviewed personnel.
Based on the results of this inspection, one self-revealing finding of very low safety significance (Green), which was determined not to involve a violation of NRC requirements, was identified.
If you contest any Non-Cited Violation (NCV) in this report, you should provide a response within 30 days of the date of this inspection report, with the basis for your denial, to the U.S. Nuclear Regulatory Commission, ATTN: Document Control Desk, Washington, DC 20555-0001; with copies to the Regional Administrator, Region III; the Director, Office of Enforcement, U.S. Nuclear Regulatory Commission, Washington, DC 20555-0001; and the NRC Resident Inspector at Clinton Power Station. In accordance with 10 CFR 2.390 of the NRCs Rules of Practice, a copy of this letter, its enclosure, and your response (if any) will be available electronically for public inspection in the NRC Public Document Room or from the Publicly Available Records (PARS) component of NRCs document system (ADAMS), accessible from the NRC Website at http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room).
Sincerely,
/RA/
Mark A. Ring, Chief Branch 1 Division of Reactor Projects Docket No. 50-461 License No. NPF-62 Enclosure:
Inspection Report No. 05000461/2006004 w/Attachment: Supplemental Information cc w/encl:
Site Vice President - Clinton Power Station Plant Manager - Clinton Power Station Regulatory Assurance Manager - Clinton Power Station Chief Operating Officer Senior Vice President - Nuclear Services Vice President - Operations Support Vice President - Licensing and Regulatory Affairs Manager Licensing - Clinton Power Station Senior Counsel, Nuclear, Mid-West Regional Operating Group Document Control Desk - Licensing Assistant Attorney General Illinois Emergency Management Agency State Liaison Officer, State of Illinois Chairman, Illinois Commerce Commission
SUMMARY OF FINDINGS
IR 05000461/2006004; AmerGen Energy Company LLC, 04/01/2006-06/30/2006; Clinton
Power Station; Event Follow-up.
This report covers a 3-month period of baseline resident inspection. The inspection was conducted by the resident inspectors. One Green finding was identified. The significance of most findings is indicated by their color (Green, White, Yellow, Red) using Inspection Manual Chapter (IMC) 0609, Significance Determination Process (SDP). Findings for which the SDP does not apply may be Green or be assigned a severity level after NRC management review.
The NRCs program for overseeing the safe operation of commercial nuclear power reactors is described in NUREG-1649, Reactor Oversight Process, Revision 3, dated July 2000.
NRC-Identified and Self-Revealing Findings
Cornerstone: Initiating Events
- Green.
On March 20, 2006, a finding of very low safety significance was self-revealed during an event. Clinton experienced a reactor scram due to a generator trip/lock out caused by an actuation of the generator differential overcurrent relay as a result of an open circuit on the C phase of the generator output current transformer. The open circuit was caused by burnt wires that resulted from inadequate workmanship, leaving terminal screws loose, following testing performed during the refueling outage in April 2002. The licensee checked all of the screws in the current transformer circuitry to ensure no others were loose, and implemented a temporary configuration change to remove the damaged phase from the circuitry. The licensee has scheduled replacement of the circuitry during the next refueling outage.
The finding was more than minor because it affected the Reactor Safety/Initiating Events cornerstone objective of limiting the likelihood of those events that upset plant stability. The finding was of very low safety significance because it did not affect the availability or function of mitigating systems. No violation of NRC requirement occurred. (Section 4OA3)
Licensee-Identified Violations
No findings of significance were identified.
REPORT DETAILS
Summary of Plant Status
The plant operated at approximately 96 percent rated thermal power (maintaining 104 percent electrical output) throughout the inspection period, with one brief reduction in power on May 21, 2006, to 79 percent, for a control rod sequence exchange.
REACTOR SAFETY
Cornerstone: Initiating Events, Mitigating Systems, and Barrier Integrity
1R04 Equipment Alignment
.1 Partial Walkdowns
a. Inspection Scope
The inspectors performed partial walkdowns of accessible portions of divisions of risk-significant mitigating systems equipment during times when the divisions were of increased importance due to the redundant divisions or other related equipment being unavailable. The inspectors utilized the valve and electric breaker checklists listed in the to verify that the components were properly positioned and that support systems were lined up as needed. The inspectors also examined the material condition of the components and observed operating parameters of equipment to verify that there were no obvious deficiencies. The inspectors reviewed outstanding work orders and issue reports associated with the divisions to verify that those documents did not reveal issues that could affect division function. The inspectors used the information in the appropriate sections of the updated safety analysis report to determine the functional requirements of the systems. The documents listed at the end of this report were also used by the inspectors to evaluate this area. The inspectors performed four samples by verifying the alignment of the following divisions:
- Division 2 emergency diesel generator and support systems;
- Division 2 shutdown service water system;
- Division 1 essential switchgear cooling system; and
- Standby liquid control system following maintenance and testing.
b. Findings
No findings of significance were identified.
.2 Complete Walkdown
a. Inspection Scope
The inspectors conducted a complete system alignment inspection of the reactor core isolation cooling system. This system was selected based on its high risk significance and mitigating systems function. The inspectors reviewed plant procedures, drawings, and the updated safety analysis report to identify proper system alignment and visually inspected system valves, instrumentation, and electrical supplies to verify proper alignment, component accessibility, availability, and current material condition. The inspectors also completed a review of corrective action documents, work orders, and operator work around and challenges to ensure there were no current operability concerns with the system. Documents reviewed during this inspection are listed in the
. These activities completed one inspection sample.
b. Findings
No findings of significance were identified.
1R05 Fire Protection
a. Inspection Scope
The inspectors conducted fire protection walkdowns which were focused on availability, accessibility, and the condition of fire fighting equipment, the control of transient combustibles and ignition sources, and on the condition and operating status of installed fire barriers. The inspectors selected fire areas for inspection based on their overall contribution to internal fire risk, as documented in the individual plant examination of external events with later additional insights, their potential to impact equipment which could cause a plant transient, or their impact on the licensees ability to respond to a security event. The inspectors used the documents listed at the end of this report to verify that fire hoses and extinguishers were in their designated locations and available for immediate use, that fire detectors and sprinklers were not obstructed, that transient material loading was within the analyzed limits, and that fire doors, dampers, and penetration seals appeared to be in satisfactory condition. The inspectors verified that minor issues identified during the inspection were entered into the licensees corrective action program.
The inspectors reviewed portions of the licensees fire protection evaluation report and the updated safety analysis report to verify consistency in the documented analysis with installed fire protection equipment at the station.
The inspectors completed seven samples by inspection of the following areas:
- Fire zone F-1m, fuel building elevation 737' 0" general access;
- Fire zone F-1a, fuel building elevation 712' 0" general access;
- Fire zone F-1b, fuel building elevation 712' 0" high pressure core spray room;
- Fire zone T-1a, turbine building elevation 712' 0" general access;
- Fire zone T-1b, condensate booster pump room;
- Fire zone CB-5a, division 3 essential switch gear area; and
- Fire zone CB-6a, control building elevation 800' 0" main control room complex.
b. Findings
No findings of significance were identified.
1R06 Flood Protection Measures
.1 Internal Flooding
a. Inspection Scope
The inspectors verified that flooding mitigation plans and equipment were consistent with the design requirements and risk analysis assumptions. The inspectors reviewed the updated safety analysis report section 3.4.1 for internal flooding events and reviewed condition reports and work orders to complete one inspection sample on the following:
- Low pressure core spray room
b. Findings
No findings of significance were identified.
1R11 Licensed Operator Requalification Program
.1 Resident Inspector Quarterly Review
a. Inspection Scope
The inspectors reviewed licensed-operator requalification training to evaluate operator performance in mitigating the consequences of a simulated event, particularly in the areas of human performance. The inspectors evaluated operator performance attributes which included communication clarity and formality, timely performance of appropriate operator actions, appropriate alarm response, proper procedure use and adherence, and senior reactor operator oversight and command and control.
Crew performance in these areas was compared to licensee management expectations and guidelines as presented in the following documents:
- OP-AA-101-111, Roles and Responsibilities of On-Shift Personnel, Revision 0;
- OP-AA-103-102, Watchstanding Practices, Revision 2;
- OP-AA-104-101, Communications, Revision 1; and
- OP-AA-106-101, Significant Event Reporting, Revision 2.
The inspectors also assessed the performance of the training staff evaluators involved in the requalification process. For any weaknesses identified, the inspectors observed that the licensee evaluators also noted the issues and discussed them in the critique at the end of the session. The inspectors verified all issues were captured in the training program and licensee corrective action process.
These activities completed one inspection sample.
b. Findings
No findings of significance were identified.
1R12 Maintenance Effectiveness
a. Inspection Scope
The inspectors reviewed the effectiveness of the licensees maintenance efforts in implementing 10 CFR 50.65 (the maintenance rule (MR)) requirements, including a review of scoping, goal-setting, performance monitoring, short and long-term corrective actions, and current equipment performance problems. These systems were selected based on their designation as risk-significant under the maintenance rule, or being in the increased monitoring (MR category (a)(1)) group. In addition, the inspectors interviewed the system engineers and maintenance rule coordinator. The inspectors also reviewed condition reports and associated documents for appropriate identification of problems, entry into the corrective action system, and appropriateness of planned or completed actions. The documents reviewed are listed at the end of the report. The inspectors completed two samples by reviewing the following:
- Division 3 essential switchgear room cooling system; and
- Containment monitoring system.
b. Findings
No findings of significance were identified.
1R13 Maintenance Risk Assessments and Emergent Work Control
a. Inspection Scope
The inspectors observed the licensees risk assessment processes and considerations used to plan and schedule maintenance activities on safety-related structures, systems, and components, particularly to ensure that maintenance risk and emergent work contingencies had been identified and resolved. The inspectors completed seven samples by assessing the effectiveness of risk management activities for the following work activities or work weeks:
- Reviewed licensees risk assessment for the high pressure core spray surveillance testing in-coincidence with reactor recirculation B hydraulic power unit filter change-out and P850 annunciator power supply replacement;
- Reviewed licensees risk assessment for upcoming standby liquid control pump maintenance;
- Reviewed licensees risk assessment for work week schedule including a control room ventilation system outage, off-gas drain trap troubleshooting, and control rod drive pump maintenance;
- Reviewed the licensees online risk assessment following entry into technical specification limiting condition for operation section 3.8.1 for failed power supply in the reserve auxiliary transformer interface panel;
- Reviewed licensees risk assessment for division 2 essential switch gear cooling being out of service due to planned cooler maintenance;
- Reviewed licensees work schedule and risk assessment for upcoming surveillance and maintenance activities on the reactor core isolation cooling system; and
- Reviewed licensees risk assessment of planned maintenance activities while experiencing pressure oscillations on discharge of the electro hydraulic control system.
b. Findings
No findings of significance were identified.
1R15 Operability Evaluations
a. Inspection Scope
The inspectors reviewed the following operability determinations and evaluations affecting mitigating systems to determine whether operability was properly justified and the component or system remained available such that no unrecognized risk increase had occurred. The inspectors completed seven samples of operability determinations and evaluations by reviewing the following:
- Operability assessment contained in issue reports 489591 and 491717, regarding reactor core isolation coolings failure at low speed/low flow operation;
- Operability assessment contained in issue report 487662, safety system annunciator power supply 1H13-P630 degraded;
- Disposition of three NRC identified issues related to high pressure core spray; issue report 483115, seal wire separated for relief valve 1E22-F035, and issue report 487297, high pressure core spray acceptance criteria;
- Licensees issue reports to assess the operability of the drywell floor drain system. Issue reports included: 496091, 1RF04T Hi-Hi Level alarm comes in before 1RF04PA starts; 482772, CPS 9543.09 Failed to work as written; and 484621, Incorrect counter number recorded during the performance of CPS 9543.10, Drywell Floor Drain Sump Level (1E31-N764) Channel Functional Test;
- Operability evaluation 472259-02 for reactor water level setpoint calculations cause inaccurate automatic trip module settings;
- Operability evaluation 491911 for divisions 1 and 3 essential switchgear cooling unit, wrong code classification for condensing unit drain piping; and
- Operability evaluation 501926 for control room ventilation damper 0VC09YB, cracked weld on crank arm to blade shaft.
b. Findings
No findings of significance were identified.
1R19 Post Maintenance Testing
a. Inspection Scope
The inspectors reviewed the post maintenance testing activities associated with maintenance or modification of important mitigating, barrier integrity, and support systems that were identified as risk significant in the licensees risk analysis. The inspectors reviewed these activities to verify that the post maintenance testing was performed adequately, demonstrated that the maintenance was successful, and that operability was restored. During this inspection activity, the inspectors interviewed maintenance and engineering department personnel and reviewed the completed post maintenance testing documentation. The inspectors used the appropriate sections of the technical specifications and updated safety analysis report, as well as the documents listed at the end of this report, to evaluate this area.
Testing subsequent to the following activities was observed and evaluated to complete three inspection samples:
- 4160 volt bus 1B1 sync-check relay after adjustment of the calibration of the emergency reserve auxilary transformer relay;
- Reactor core isolation cooling system troubleshooting after failing the in-service inspection portion of its quarterly surveillance; and
- Control room ventilation train A, hydramotor replacements and preventative maintenance.
b. Findings
No findings of significance were identified.
1R22 Surveillance Testing
a. Inspection Scope
The inspectors witnessed selected surveillance tests and/or reviewed test data to verify that the equipment tested using the surveillance procedures met the technical specifications, the operations requirements manual, the updated safety analysis report, and licensee procedural requirements, and demonstrated that the equipment was capable of performing its intended safety functions. The activities were selected based on their importance in verifying mitigating systems capability and barrier integrity. The inspectors used the documents listed at the end of this report to verify that the testing met the frequency requirements; that the tests were conducted in accordance with the procedures, including establishing the proper plant conditions and prerequisites; that the test acceptance criteria were met; and that the results of the tests were properly reviewed and recorded. In addition, the inspectors interviewed operations, maintenance and engineering department personnel regarding the tests and test results.
The inspectors completed two samples of reactor coolant system leakage detection surveillances by evaluating the following activities:
- CPS 9000.01D001, Control Room Surveillance Log Mode 1, 2, 3 Data Sheet, section 8.9, Reactor Coolant System - Operational Leakage; and
The inspectors completed five samples of in-service testing activities by evaluating the following surveillance tests:
- CPS 9051.02, High Pressure Core Spray Valve Operability Test;
- CPS 9054.01, Reactor Core Isolation Cooling System Operability Check;
- CPS 9069.01, Shutdown Service Water Operability Test;
- CPS 9051.01, High Pressure Core Spray Pump and High Pressure Core Spray Water Leg Pump Operability; and
- CPS 9015.01, Standby Liquid Control System Operability.
b. Findings
No findings of significance were identified.
Cornerstone: Emergency Preparedness
1EP6 Drill Evaluation
a. Inspection Scope
The inspectors observed the emergency response activities associated with the drill conducted on May 23, 2006. Specifically, the inspectors verified that the emergency classification and simulated notifications were properly completed, and that the licensee adequately critiqued the training. Additionally, the inspectors observed licensee activities during the drill in the new technical support center, and attended the post-drill critique. The inspectors discussed drill discrepancies with the emergency preparedness manager. The inspectors completed one inspection sample by observing the following emergency drill:
- High drywell pressure and lowering reactor pressure vessel level.
b. Findings
No findings of significance were identified.
OTHER ACTIVITIES
4OA1 Performance Indicator Verification
Cornerstone: Initiating Events
a. Inspection Scope
The inspectors sampled the licensees submittals for performance indicators for the period of April 2004 through March 2006. The inspectors used performance indicator definitions and guidance contained in revision 4 of Nuclear Energy Institute (NEI)document 99-02, Regulatory Assessment Performance Indicator Guideline to verify the accuracy of the performance indicator data. The inspectors performed three samples by reviewing the following:
- Scrams with Loss of Normal Heat Removal;
- Unplanned Scrams per 7,000 Critical Hours; and
- Unplanned Power Changes per 7,000 Critical Hours.
b. Findings
No findings of significance were identified.
4OA2 Identification and Resolution of Problems
a. Inspection Scope
As discussed in previous sections of this report, the inspectors routinely reviewed issues during baseline inspection activities and plant status reviews to verify that they were being entered into the licensees corrective action system at an appropriate threshold, that adequate attention was being given to timely corrective actions, and that adverse trends were identified and addressed. Minor issues entered into the licensees corrective action system as a result of inspectors observations are generally denoted in the report.
b. Findings
No findings of significance were identified.
4OA3 Event Follow-up
.1 (Closed) Licensee Event Report 05000461/2006-01:
Failure to tighten terminal screw causes turbine/generator trip and reactor scram.
a. Inspection Scope
The inspectors reviewed the licensee event report and issue report 468357, which documented this event in the corrective action program, to verify that the cause of the event was identified and to verify that the corrective actions addressed the root cause of this event.
b. Findings
Introduction:
A self-revealed Green finding was identified when a loose terminal screw on the C phase neutral current transformer of the main generator output caused the generator differential overcurrent 87-G1 relay to trip due to a sensed current imbalance resulting in a turbine/generator trip and reactor scram.
Description:
On March 20, 2006, Clinton experienced a reactor scram due to an open circuit in the C phase neutral current transformer of the main generator output. This open circuit caused the generator differential overcurrent 87-G1 relay to trip due to a sensed current imbalance. Actuation of the 87-G1 relay resulted in a generator trip/lockout and an automatic turbine electro hydraulic control trip. The turbine electro hydraulic control trip caused a turbine control valve fast closure and a reactor protection signal for the automatic scram. The licensees troubleshooting team traced the open circuit on the C phase neutral current transformer to a junction box under the main generator. The licensee determined that the open circuit was likely due to a loose terminal screw on the current transformer lead wire. This loose screw resulted in high resistance and overheating of the wire. The licensee implemented a temporary modification, TCCP# 360128, to remove the failed current transformer and disable the input to the 87-G1 relay. A permanent repair/replacement was planned for the next refueling outage.
The licensee conducted a root cause investigation to determine why the terminal screw was loose on the current transformer. Vibration was ruled out because vibration appeared to be low in the junction boxes and the friction in the terminals was significant.
During the investigation, only 3 of the 60 screws in the current transformer systems were found to be backed-off. The root cause team was unable to identify a specific work activity that caused the loose screw, but determined that inadequate workmanship was the cause of the loose screw. The licensee checked all of the current transformer circuits for loose screws. The screw that caused the event and two others on the same circuit were the only screws found loose on the current transformer circuits. The licensee determined this condition was caused by a task that involved temporary shorting of the circuit during testing, and when the test leads were removed, the loose screws were not re-tightened adequately. Through a work history search, the licensee determined the most likely time for the screws to be left loose was during hi-pot testing on April 25, 2002, performed under work order 332675. The licensees review of these work documents revealed that site procedures were probably not followed in this activity since there were no lifted and landed leads forms in the work package and no specific steps to ground the current transformer leads. Licensee interviews of General Electric (GE) personnel and review of GE procedures indicated that current transformer grounding was required for hi-pot testing, although there was no documentation showing that this was done. The licensee created a corrective action to revise the pre-outage checklist to require verification that all lifted and landed leads activities in support of GE work are properly added to the work order packages and to require briefing workers before the outage begins to reinforce the expectations on lifted and landed leads work.
Analysis:
The inspectors considered the failure to adequately tighten terminal screws in the main generator output current transformer circuit a performance deficiency. This issue was caused by inadequate workmanship. The inspectors used IMC 0612, Appendix B, to disposition this issue and determined it was more than minor because the finding affected the reactor safety/initiating events cornerstone objective of limiting the likelihood of those events that upset plant stability. The finding also affected the cross-cutting area of human performance because the contract workers failed to tighten the terminal screws of the current transformer and the licensee failed to ensure the GE workers were using the appropriate lifted and landed leads documents to aid in performance of this job. Although this failure occurred in C1R08 in April, 2002, the inspectors determined this deficiency to be reflective of recent licensee performance because, up to the March 2006 scram event, there was no procedure or process in place to ensure GE followed the licensees lifted and landed lead procedures. As a result of the root cause for this event, the licensee initiated a corrective action to revise the GE quality control check-list to confirm that requirements similar to wire removal/jumper installation procedures are incorporated. The inspectors evaluated this finding using IMC 0609, Significance Determination Process, Appendix A, Significance Determination of Reactor Inspection Findings for At-Power Situations, Phase 1 screening associated with the initiating events cornerstone. Although this finding did contribute to the likelihood of a reactor trip, it did not affect the function or availability of any mitigation equipment. Therefore, the inspectors concluded that this issue was a finding of very low safety significance (Green).
Enforcement:
Though the inadequate workmanship that occurred during generator high-potential testing was a performance deficiency, no violation of regulatory requirements occurred. This issue was considered a finding of very low safety significance (FIN 05000461/2006004-01). This issue was documented in the licensees corrective action program as issue report 468357, Reactor Scram Due to Main Turbine/Generator Trip.
4OA6 Meetings
.1 Exit Meeting
The inspectors presented the inspection results to Mr. B. Hanson and other members of licensee management at the conclusion of the inspection on July 13, 2006. The inspectors asked the licensee whether any materials examined during the inspection should be considered proprietary. No proprietary information was identified.
ATTACHMENT:
SUPPLEMENTAL INFORMATION
KEY POINTS OF CONTACT
Licensee personnel
- B. Hanson, Site Vice President
- M. McDowell, Plant Manager
- J. Cunningham, Work Management Director
- J. Stovall, Outage Manager
- G. Vickers, Radiation Protection Director
- R. Frantz, Regulatory Assurance Representative
- M. Hiter, Access Control Supervisor
- P. Simpson, Regulatory Assurance Director (Acting)
- C. Vandenburgh, Nuclear Oversight Manager
- J. Domitrovich, Maintenance Director
- D. Schavey, Operations Director
- R. Campbell, Chemistry Manager (Acting)
- J. Lindsay, Training Manager
- C. Williamson, Security Manager
- R. Peak, Site Engineering Director
- T. Chalmers, Shift Operations Superintendent
LIST OF ITEMS
OPENED, CLOSED AND DISCUSSED
Opened and Closed
- 05000461/2006004-01 FIN Failure to tighten terminal screw causes turbine/generator trip and reactor scram due to inadequate workmanship.
- 05000461/2006-01 LER Failure to tighten terminal screw causes turbine/generator trip and reactor scram.
Discussed
None.