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River Bend Station
River Bend Station
5485 US Highway 61N
5485 US Highway 61N
St. Francisville, LA 70775
St. Francisville, LA 70775
SUBJECT:       RIVER BEND STATION - NRC INTEGRATED INSPECTION
SUBJECT:
                REPORT 05000458/2006003
RIVER BEND STATION - NRC INTEGRATED INSPECTION
REPORT 05000458/2006003
Dear Mr. Hinnenkamp:
Dear Mr. Hinnenkamp:
On June 30, 2006, the U.S. Nuclear Regulatory Commission (NRC) completed an inspection at
On June 30, 2006, the U.S. Nuclear Regulatory Commission (NRC) completed an inspection at
your River Bend Station. The enclosed integrated inspection report documents the inspection
your River Bend Station. The enclosed integrated inspection report documents the inspection
results, which were discussed on July 5, 2006, with you and other members of your staff.
results, which were discussed on July 5, 2006, with you and other members of your staff.
The inspection examined activities conducted under your license as they relate to safety and
The inspection examined activities conducted under your license as they relate to safety and
compliance with the Commissions rules and regulations and with the conditions of your license.
compliance with the Commissions rules and regulations and with the conditions of your license.  
The inspectors reviewed selected procedures and records, observed activities, and interviewed
The inspectors reviewed selected procedures and records, observed activities, and interviewed
personnel.
personnel.
The report documents three NRC-identified findings and two self-revealing findings of very low
The report documents three NRC-identified findings and two self-revealing findings of very low
safety significance (Green). The NRC has also determined that violations are associated with
safety significance (Green). The NRC has also determined that violations are associated with
these findings. However, because these violations were of very low safety significance and
these findings. However, because these violations were of very low safety significance and
were entered into your corrective action program, the NRC is treating these violations as
were entered into your corrective action program, the NRC is treating these violations as
noncited violations, consistent with Section VI.A.1 of the NRC Enforcement Policy. If you
noncited violations, consistent with Section VI.A.1 of the NRC Enforcement Policy. If you
contest the violations or the significance of the violations, you should provide a response within
contest the violations or the significance of the violations, you should provide a response within
30 days of the date of this inspection report, with the basis for your denial, to the U.S. Nuclear
30 days of the date of this inspection report, with the basis for your denial, to the U.S. Nuclear
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enclosure, and your response (if any) will be available electronically for public inspection in the
enclosure, and your response (if any) will be available electronically for public inspection in the
NRC Public Document Room or from the Publicly Available Records (PARS) component of
NRC Public Document Room or from the Publicly Available Records (PARS) component of
NRCs document system (ADAMS). ADAMS is accessible from the NRC Website at
NRCs document system (ADAMS). ADAMS is accessible from the NRC Website at
http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room).
http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room).


Entergy Operations, Inc.                 -2-
Entergy Operations, Inc.
-2-
Should you have any questions concerning this inspection, we will be pleased to discuss them
Should you have any questions concerning this inspection, we will be pleased to discuss them
with you.
with you.
                                        Sincerely,
Sincerely,
                                                /RA/
/RA/
                                        Kriss M. Kennedy, Chief
Kriss M. Kennedy, Chief
                                        Project Branch C
Project Branch C
                                        Division of Reactor Projects
Division of Reactor Projects
Docket: 50-458
Docket:   50-458
License: NPF-47
License: NPF-47
Enclosure:
Enclosure:
NRC Inspection Report 05000458/2006003
NRC Inspection Report 05000458/2006003
  w/Attachment: Supplemental Information
  w/Attachment: Supplemental Information
cc w/enclosure:
cc w/enclosure:
Senior Vice President and
Senior Vice President and  
Chief Operating Officer
  Chief Operating Officer
Entergy Operations, Inc.
Entergy Operations, Inc.
P.O. Box 31995
P.O. Box 31995
Jackson, MS 39286-1995
Jackson, MS 39286-1995
Vice President
Vice President  
Operations Support
Operations Support
Entergy Operations, Inc.
Entergy Operations, Inc.
P.O. Box 31995
P.O. Box 31995
Jackson, MS 39286-1995
Jackson, MS 39286-1995
General Manager
General Manager
Plant Operations
Plant Operations
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River Bend Station
River Bend Station
5485 US Highway 61N
5485 US Highway 61N
St. Francisville, LA 70775
St. Francisville, LA 70775
Director - Nuclear Safety
Director - Nuclear Safety
Entergy Operations, Inc.
Entergy Operations, Inc.
River Bend Station
River Bend Station
5485 US Highway 61N
5485 US Highway 61N
St. Francisville, LA 70775
St. Francisville, LA 70775
Wise, Carter, Child & Caraway
Wise, Carter, Child & Caraway
P.O. Box 651
P.O. Box 651
Jackson, MS 39205
Jackson, MS 39205


Entergy Operations, Inc.             -3-
Entergy Operations, Inc.
-3-
Winston & Strawn LLP
Winston & Strawn LLP
1700 K Street, N.W.
1700 K Street, N.W.
Washington, DC 20006-3817
Washington, DC 20006-3817
Manager - Licensing
Manager - Licensing
Entergy Operations, Inc.
Entergy Operations, Inc.
River Bend Station
River Bend Station
5485 US Highway 61N
5485 US Highway 61N
St. Francisville, LA 70775
St. Francisville, LA 70775
The Honorable Charles C. Foti, Jr.
The Honorable Charles C. Foti, Jr.
Attorney General
Attorney General
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State of Louisiana
State of Louisiana
P.O. Box 94005
P.O. Box 94005
Baton Rouge, LA 70804-9005
Baton Rouge, LA 70804-9005
H. Anne Plettinger
H. Anne Plettinger
3456 Villa Rose Drive
3456 Villa Rose Drive
Baton Rouge, LA 70806
Baton Rouge, LA 70806
Bert Babers, President
Bert Babers, President
West Feliciana Parish Police Jury
West Feliciana Parish Police Jury
P.O. Box 1921
P.O. Box 1921
St. Francisville, LA 70775
St. Francisville, LA 70775
Richard Penrod, Senior Environmental
Richard Penrod, Senior Environmental  
Scientist
  Scientist
Office of Environmental Services
Office of Environmental Services
Northwestern State University
Northwestern State University  
Russell Hall, Room 201
Russell Hall, Room 201
Natchitoches, LA 71497
Natchitoches, LA 71497
Brian Almon
Brian Almon
Public Utility Commission
Public Utility Commission
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P.O. Box 13326
P.O. Box 13326
1701 North Congress Avenue
1701 North Congress Avenue
Austin, TX 78711-3326
Austin, TX 78711-3326


Entergy Operations, Inc.           -4-
Entergy Operations, Inc.
-4-
Chairperson
Chairperson
Denton Field Office
Denton Field Office  
Chemical and Nuclear Preparedness
Chemical and Nuclear Preparedness  
  and Protection Division
  and Protection Division
Office of Infrastructure Protection
Office of Infrastructure Protection
Preparedness Directorate
Preparedness Directorate
Line 136: Line 140:
800 North Loop 288
800 North Loop 288
Federal Regional Center
Federal Regional Center
Denton, TX 76201-3698
Denton, TX 76201-3698


Entergy Operations, Inc.                   -5-
Entergy Operations, Inc.
-5-
Electronic distribution by RIV:
Electronic distribution by RIV:
Regional Administrator (BSM1)
Regional Administrator (BSM1)
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RBS Site Secretary (LGD)
RBS Site Secretary (LGD)
W. A. Maier, RSLO (WAM)
W. A. Maier, RSLO (WAM)
SUNSI Review Completed: __wcw_ ADAMS: : Yes G No                 Initials: __wcw___
SUNSI Review Completed: __wcw_     ADAMS: : Yes
: Publicly Available      G Non-Publicly Available G Sensitive   : Non-Sensitive
G No           Initials: __wcw___  
R:\_REACTORS\_RB\2006\RB2006-03RP-PJA.wpd
:   Publicly Available      G   Non-Publicly Available     G   Sensitive
RIV:SRI:DRP/C         RI:DRP/C       C:DRS/OB       C:DRS/EB1       C:DRS/PSB
:   Non-Sensitive
PJAlter               MOMiller       ATGody         JAClark         MPShannon
R:\\_REACTORS\\_RB\\2006\\RB2006-03RP-PJA.wpd
  T - WCWalker         E - WCWalker     /RA/           /RA/             /RA/
RIV:SRI:DRP/C
8/10/06               8/10/06         8/11/06       8/10/06         8/10/06
RI:DRP/C
C:DRS/EB2             SRA:DRS         C:DRP/C
C:DRS/OB
LJSmith               DPLoveless     KMKennedy
C:DRS/EB1
     /RA/                   /RA/             /RA/
C:DRS/PSB
8/10/06               8/14/06         8/14/06
PJAlter
OFFICIAL RECORD COPY                               T=Telephone     E=E-mail     F=Fax
MOMiller
ATGody
JAClark
MPShannon
  T - WCWalker
E - WCWalker
  /RA/
    /RA/
      /RA/
8/10/06
8/10/06
8/11/06
8/10/06
8/10/06
C:DRS/EB2
SRA:DRS
C:DRP/C
LJSmith
DPLoveless
KMKennedy
     /RA/
    /RA/
    /RA/
8/10/06
8/14/06
8/14/06
OFFICIAL RECORD COPY  
T=Telephone           E=E-mail       F=Fax


              U.S. NUCLEAR REGULATORY COMMISSION
Enclosure
                                  REGION IV
-1-
Docket:     50-458
U.S. NUCLEAR REGULATORY COMMISSION
License:     NPF-47
REGION IV
Report:     05000458/2006003
Docket:
Licensee:   Entergy Operations, Inc.
50-458
Facility:   River Bend Station
License:
Location:   5485 U.S. Highway 61
NPF-47
            St. Francisville, Louisiana
Report:
Dates:       April 1 to June 30, 2006
05000458/2006003
Inspectors: P. Alter, Senior Resident Inspector, Project Branch C
Licensee:
            M. Miller, Resident Inspector, Project Branch C
Entergy Operations, Inc.
            G. Werner, Senior Project Engineer, Project Branch D
Facility:
            L. Ricketson, P.E., Senior Health Physicist, Plant Support Branch
River Bend Station
            W. Sifre, Senior Reactor Inspector, Engineering Branch 1
Location:
Approved By: Kriss M. Kennedy, Chief
5485 U.S. Highway 61
            Project Branch C
St. Francisville, Louisiana
            Division of Reactor Projects
Dates:
                                      -1-                                  Enclosure
April 1 to June 30, 2006
Inspectors:
P. Alter, Senior Resident Inspector, Project Branch C
M. Miller, Resident Inspector, Project Branch C
G. Werner, Senior Project Engineer, Project Branch D
L. Ricketson, P.E., Senior Health Physicist, Plant Support Branch
W. Sifre, Senior Reactor Inspector, Engineering Branch 1
Approved By:
Kriss M. Kennedy, Chief
Project Branch C
Division of Reactor Projects


                                      TABLE OF CONTENTS
Enclosure
-2-
TABLE OF CONTENTS
SUMMARY OF FINDINGS . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 3
SUMMARY OF FINDINGS . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 3
REPORT DETAILS . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 6
REPORT DETAILS . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 6
REACTOR SAFETY . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 6
REACTOR SAFETY . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 6
      1R01 Adverse Weather Protection . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 6
1R01
      1R04 Equipment Alignment . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 7
Adverse Weather Protection . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 6
      1R05 Fire Protection . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 7
1R04
      1R08 Inservice Inspection Activities . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 8
Equipment Alignment . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 7
      1R11 Licensed Operator Requalification Program . . . . . . . . . . . . . . . . . . . . . . . . . . . 9
1R05
      1R12 Maintenance Effectiveness . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 10
Fire Protection . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 7
      1R13 Maintenance Risk Assessments and Emergent Work Control . . . . . . . . . . . . . 10
1R08
      1R14 Operator Performance During Nonroutine Evolutions and Events . . . . . . . . . . 11
Inservice Inspection Activities . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 8
      1R15 Operability Evaluations . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 12
1R11
      1R19 Postmaintenance Testing . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 17
Licensed Operator Requalification Program . . . . . . . . . . . . . . . . . . . . . . . . . . . 9
      1R20 Refueling and Other Outage Activities . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 17
1R12
      1R22 Surveillance Testing . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 20
Maintenance Effectiveness . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 10
      1R23 Temporary Plant Modifications . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 23
1R13
      1EP6 Drill Evaluation . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 23
Maintenance Risk Assessments and Emergent Work Control . . . . . . . . . . . . . 10
1R14
Operator Performance During Nonroutine Evolutions and Events . . . . . . . . . . 11
1R15
Operability Evaluations . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 12
1R19
Postmaintenance Testing . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 17
1R20
Refueling and Other Outage Activities . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 17
1R22
Surveillance Testing
. . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 20
1R23
Temporary Plant Modifications
. . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 23
1EP6 Drill Evaluation . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 23
RADIATION SAFETY . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 24
RADIATION SAFETY . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 24
      2OS1 Access Control to Radiologically Significant Areas . . . . . . . . . . . . . . . . . . . . . 24
2OS1 Access Control to Radiologically Significant Areas . . . . . . . . . . . . . . . . . . . . . 24
      2OS2 ALARA Planning and Controls . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 27
2OS2 ALARA Planning and Controls . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 27
OTHER ACTIVITIES . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 28
OTHER ACTIVITIES . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 28
      4OA1 Performance Indicator (PI) Verification . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 28
4OA1 Performance Indicator (PI) Verification . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 28
      4OA2 Identification and Resolution of Problems . . . . . . . . . . . . . . . . . . . . . . . . . . . . 29
4OA2 Identification and Resolution of Problems . . . . . . . . . . . . . . . . . . . . . . . . . . . . 29
      4OA3 Event Followup . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 31
4OA3 Event Followup . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 31
      4OA5 Other Activities . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 32
4OA5 Other Activities . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 32
      4OA6 Meetings, Including Exit . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 32
4OA6 Meetings, Including Exit . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 32
SUPPLEMENTAL INFORMATION . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . A-1
SUPPLEMENTAL INFORMATION . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . A-1
KEY POINTS OF CONTACT . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . A-1
KEY POINTS OF CONTACT . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . A-1
Line 219: Line 278:
LIST OF DOCUMENTS REVIEWED . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . A-2
LIST OF DOCUMENTS REVIEWED . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . A-2
LIST OF ACRONYMS . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . A-7
LIST OF ACRONYMS . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . A-7
                                                        -2-                                                          Enclosure


                                    SUMMARY OF FINDINGS
Enclosure
-3-
SUMMARY OF FINDINGS
IR 05000458/2006003; 04/01/2006 - 06/30/2006; River Bend Station; Operability Evaluations,
IR 05000458/2006003; 04/01/2006 - 06/30/2006; River Bend Station; Operability Evaluations,
Refueling and Other Outage Activities, Surveillance Testing, Occupational Radiation Safety.
Refueling and Other Outage Activities, Surveillance Testing, Occupational Radiation Safety.
The report covered a 3-month period of routine baseline inspections by resident inspectors and
The report covered a 3-month period of routine baseline inspections by resident inspectors and
announced baseline inspections by regional engineering and radiation protection inspectors.
announced baseline inspections by regional engineering and radiation protection inspectors.  
Five Green noncited violations were identified. The significance of most findings is indicated by
Five Green noncited violations were identified. The significance of most findings is indicated by
their color (Green, White, Yellow, Red) using Inspection Manual Chapter 0609, Significance
their color (Green, White, Yellow, Red) using Inspection Manual Chapter 0609, Significance
Determination Process. Findings for which the significance determination process does not
Determination Process. Findings for which the significance determination process does not
apply may be Green or be assigned a severity level after NRC management review. The
apply may be Green or be assigned a severity level after NRC management review. The
NRCs program for overseeing the safe operation of commercial nuclear power reactors is
NRCs program for overseeing the safe operation of commercial nuclear power reactors is
described in NUREG-1649, Reactor Oversight Process, Revision 3, dated July 2000.
described in NUREG-1649, Reactor Oversight Process, Revision 3, dated July 2000.
A.     NRC-Identified and Self-Revealing Findings
A.
Cornerstone: Mitigating Systems
NRC-Identified and Self-Revealing Findings
        Green. A self-revealing noncited violation of 10 CFR Part 50, Appendix B, Criterion XVI,
Cornerstone: Mitigating Systems
        "Corrective Action," was reviewed involving the failure of the licensee to identify that the
Green. A self-revealing noncited violation of 10 CFR Part 50, Appendix B, Criterion XVI,
        normal supply breaker to the Division III 4.16 kV engineered safety features bus was not
"Corrective Action," was reviewed involving the failure of the licensee to identify that the
        properly racked in for a period of 24 days following maintenance. This issue was
normal supply breaker to the Division III 4.16 kV engineered safety features bus was not
        entered into the licensee's corrective action program as CR-RBS-2006-02402.
properly racked in for a period of 24 days following maintenance. This issue was
        The finding was more than minor because it was associated with the mitigating system
entered into the licensee's corrective action program as CR-RBS-2006-02402.
        cornerstone attribute of configuration control and affected the associated cornerstone
The finding was more than minor because it was associated with the mitigating system
        objective to ensure the availability, reliability, and capability of systems that respond to
cornerstone attribute of configuration control and affected the associated cornerstone
        initiating events to prevent undesirable consequences. Utilizing Manual Chapter 0609,
objective to ensure the availability, reliability, and capability of systems that respond to
        "Significance Determination Process," a Phase 3 analysis concluded that the finding
initiating events to prevent undesirable consequences. Utilizing Manual Chapter 0609,
        was of very low safety significance. The cause of the finding was related to the
"Significance Determination Process," a Phase 3 analysis concluded that the finding
        crosscutting aspect of problem identification and resolution in that the licensee failed to
was of very low safety significance. The cause of the finding was related to the
        properly evaluate available indications to identify that the breaker was not properly
crosscutting aspect of problem identification and resolution in that the licensee failed to
        racked in. (Section 1R15).
properly evaluate available indications to identify that the breaker was not properly
        Green. An NRC identified noncited violation of 10 CFR 50.65 Maintenance Rule
racked in. (Section 1R15).
        Section (a)(4) was identified for the failure of the licensee to provide prescribed
Green. An NRC identified noncited violation of 10 CFR 50.65 Maintenance Rule
        compensatory measures for two Orange shutdown risk conditions during Refueling
Section (a)(4) was identified for the failure of the licensee to provide prescribed
        Outage 13. Specifically, the preoutage risk assessment recommended that two work
compensatory measures for two Orange shutdown risk conditions during Refueling
        orders be in place for maintenance electricians to provide power to one spent fuel pool
Outage 13. Specifically, the preoutage risk assessment recommended that two work
        cooling pump in the event of problems with the running pump during periods of electrical
orders be in place for maintenance electricians to provide power to one spent fuel pool
        bus maintenance. The inspectors found that the work packages were not in place
cooling pump in the event of problems with the running pump during periods of electrical
        before entering shutdown risk condition Orange on April 26, 2006, during the Division II
bus maintenance. The inspectors found that the work packages were not in place
        engineering safety features bus testing, and May 3, 2006, during the Division I
before entering shutdown risk condition Orange on April 26, 2006, during the Division II
        engineered safety features bus outage. This issue was entered into the licensee's
engineering safety features bus testing, and May 3, 2006, during the Division I
        corrective action program as CR-RBS-2006-01937.
engineered safety features bus outage. This issue was entered into the licensee's
        The finding was more than minor because the licensee failed to implement a prescribed
corrective action program as CR-RBS-2006-01937.
        compensatory measure during the highest risk condition of Refueling Outage 13. The
The finding was more than minor because the licensee failed to implement a prescribed
                                                  -3-                                      Enclosure
compensatory measure during the highest risk condition of Refueling Outage 13. The


      specific compensatory measures were called for in the preoutage risk assessment and
Enclosure
      the shutdown operations protection plan. The finding affected the mitigating system
-4-
      cornerstone because of the increased risk of a sustained loss of spent fuel pool cooling
specific compensatory measures were called for in the preoutage risk assessment and
      during core offloading operations. The finding could not be evaluated using the
the shutdown operations protection plan. The finding affected the mitigating system
      significance determination process, therefore the finding was reviewed by regional
cornerstone because of the increased risk of a sustained loss of spent fuel pool cooling
      management and determined to be of very low safety significance. Factors that were
during core offloading operations. The finding could not be evaluated using the
      considered included: (1) electrical maintenance technicians had previously performed
significance determination process, therefore the finding was reviewed by regional
      the task of providing alternate power to a spent fuel pool cooling pump, (2) the
management and determined to be of very low safety significance. Factors that were
      necessary equipment was staged as part of the abnormal operating procedure for loss
considered included: (1) electrical maintenance technicians had previously performed
      of decay heat removal, and (3) the relatively long time to boil of the spent fuel storage
the task of providing alternate power to a spent fuel pool cooling pump, (2) the
      pool at that time during the refueling outage. The cause of the finding was related to the
necessary equipment was staged as part of the abnormal operating procedure for loss
      crosscutting aspect of human performance because the licensees planned
of decay heat removal, and (3) the relatively long time to boil of the spent fuel storage
      maintenance activities and the predetermined increase in outage risk was not effectively
pool at that time during the refueling outage. The cause of the finding was related to the
      managed by prescribed compensatory measures (Section 1R20).
crosscutting aspect of human performance because the licensees planned
      Green. An NRC identified noncited violation of Technical Specification 5.4.1.a was
maintenance activities and the predetermined increase in outage risk was not effectively
      identified for the failure of the licensee to provide an adequate surveillance test
managed by prescribed compensatory measures (Section 1R20).
      procedure to perform Technical Specification Surveillance Requirement 3.8.1.1.
Green. An NRC identified noncited violation of Technical Specification 5.4.1.a was
      Specifically, STP-000-0102, Power Distribution Alignment Check, Revision 4, did not
identified for the failure of the licensee to provide an adequate surveillance test
      verify the required offsite power circuit breaker alignment and indicated power
procedure to perform Technical Specification Surveillance Requirement 3.8.1.1.  
      availability for the Division III 4.16 kV engineered safety features bus as required in
Specifically, STP-000-0102, Power Distribution Alignment Check, Revision 4, did not
      Modes 1, 2, and 3. This issue was entered into the licensee's corrective action program
verify the required offsite power circuit breaker alignment and indicated power
      as CR-RBS-2006-02675 and -02402.
availability for the Division III 4.16 kV engineered safety features bus as required in
      The finding was more than minor because it was associated with the mitigating system
Modes 1, 2, and 3. This issue was entered into the licensee's corrective action program
      cornerstone attribute of configuration control and affected the associated cornerstone
as CR-RBS-2006-02675 and -02402.
      objective to ensure the availability, reliability, and capability of systems that respond to
The finding was more than minor because it was associated with the mitigating system
      initiating events to prevent undesirable consequences. Utilizing Manual Chapter 0609,
cornerstone attribute of configuration control and affected the associated cornerstone
      "Significance Determination Process," a Phase 3 analysis concluded that the finding
objective to ensure the availability, reliability, and capability of systems that respond to
      was of very low safety significance. (Section 1R22).
initiating events to prevent undesirable consequences. Utilizing Manual Chapter 0609,
Cornerstone: Occupational Radiation Safety
"Significance Determination Process," a Phase 3 analysis concluded that the finding
*     Green. The inspector reviewed a self-revealing noncited violation of Technical
was of very low safety significance. (Section 1R22).
      Specification 5.7.1, resulting from the licensees failure to control access to a high
Cornerstone: Occupational Radiation Safety
      radiation area. While transferring reverse osmosis system filters in the radwaste
*
      building, the licensee allowed two workers to inadvertently enter a high radiation area.
Green. The inspector reviewed a self-revealing noncited violation of Technical
      This occurred after a guard prematurely left his post in front of the 123 foot elevation
Specification 5.7.1, resulting from the licensees failure to control access to a high
      elevator door. The highest dose rate recorded by an electronic alarming dosimeter was
radiation area. While transferring reverse osmosis system filters in the radwaste
      164 millirem per hour. The guard returned and evacuated the workers before they
building, the licensee allowed two workers to inadvertently enter a high radiation area.  
      accrued additional radiation dose. Planned corrective action was still being evaluated by
This occurred after a guard prematurely left his post in front of the 123 foot elevation
      the licensee at the conclusion of the inspection.
elevator door. The highest dose rate recorded by an electronic alarming dosimeter was
      The finding was more than minor because it was associated with the occupational
164 millirem per hour. The guard returned and evacuated the workers before they  
      radiation safety attribute of exposure control and affected the cornerstone objective in
accrued additional radiation dose. Planned corrective action was still being evaluated by
      that not controlling a high radiation area could increase personal exposure. Using the
the licensee at the conclusion of the inspection.
      Occupational Radiation Safety Significance Determination Process, the inspector
The finding was more than minor because it was associated with the occupational
      determined that the finding was of very low safety significance because it did not
radiation safety attribute of exposure control and affected the cornerstone objective in
                                                -4-                                      Enclosure
that not controlling a high radiation area could increase personal exposure. Using the
Occupational Radiation Safety Significance Determination Process, the inspector
determined that the finding was of very low safety significance because it did not


  involve: (1) an as low as is reasonably achievable finding, (2) an overexposure, (3) a
Enclosure
  substantial potential for overexposure, or (4) an impaired ability to assess dose.
-5-
  Additionally, this finding had crosscutting aspects associated with human performance
involve: (1) an as low as is reasonably achievable finding, (2) an overexposure, (3) a
  in that the failure of the individual to guard the elevator door directly contributed to the
substantial potential for overexposure, or (4) an impaired ability to assess dose.  
  violation. (Section 2OS1)
Additionally, this finding had crosscutting aspects associated with human performance
* Green. The inspector identified a noncited violation of 10 CFR 20.1501(a) because the
in that the failure of the individual to guard the elevator door directly contributed to the
  license failed to survey airborne radioactivity. During the removal of local power range
violation. (Section 2OS1)
  monitors, the licensee started collecting an air sample of the work area, but discarded
*
  the sample before analyzing it. Successful passage through the portal monitors at the
Green. The inspector identified a noncited violation of 10 CFR 20.1501(a) because the
  exit of the controlled access area confirmed that no worker experienced an uptake of
license failed to survey airborne radioactivity. During the removal of local power range
  radioactive material. Planned corrective action is still being evaluated.
monitors, the licensee started collecting an air sample of the work area, but discarded
  The finding was more than minor because it was associated with the occupational
the sample before analyzing it. Successful passage through the portal monitors at the
  radiation safety program attribute of exposure control and affected the cornerstone
exit of the controlled access area confirmed that no worker experienced an uptake of
  objective in that the lack of knowledge of radiological conditions could increase
radioactive material. Planned corrective action is still being evaluated.
  personnel dose. Using the Occupational Radiation Safety Significance Determination
The finding was more than minor because it was associated with the occupational
  Process, the inspector determined that the finding was of very low safety significance
radiation safety program attribute of exposure control and affected the cornerstone
  because it did not involve: (1) an as low as is reasonably achievable finding, (2) an
objective in that the lack of knowledge of radiological conditions could increase
  overexposure, (3) a substantial potential for overexposure, or (4) an impaired ability to
personnel dose. Using the Occupational Radiation Safety Significance Determination
  assess dose. Additionally, this finding had crosscutting aspects associated with human
Process, the inspector determined that the finding was of very low safety significance
  performance in that the failure to maintain the sample for analysis directly contributed to
because it did not involve: (1) an as low as is reasonably achievable finding, (2) an
  the violation. (Section 2OS1)
overexposure, (3) a substantial potential for overexposure, or (4) an impaired ability to
B. Licensee-Identified Violations
assess dose. Additionally, this finding had crosscutting aspects associated with human
  None.
performance in that the failure to maintain the sample for analysis directly contributed to
                                              -5-                                      Enclosure
the violation. (Section 2OS1)
B.
Licensee-Identified Violations
None.


                                      REPORT DETAILS
Enclosure
Summary of Plant Status: The reactor was operated at 100 percent power from April 1-15,
-6-
REPORT DETAILS
Summary of Plant Status: The reactor was operated at 100 percent power from April 1-15,
2006, when the reactor scrammed due to a control circuit failure which caused both reactor
2006, when the reactor scrammed due to a control circuit failure which caused both reactor
recirculation pumps to shift to slow speed. The reactor was restarted on April 17 and attained
recirculation pumps to shift to slow speed. The reactor was restarted on April 17 and attained
100 percent power on April 18. On April 23, the reactor was shut down for Refueling Outage
100 percent power on April 18. On April 23, the reactor was shut down for Refueling Outage
(RFO) -13. On May 12, the reactor was restarted and attained 100 percent power on May 18.
(RFO) -13. On May 12, the reactor was restarted and attained 100 percent power on May 18.  
On June 15, reactor power was reduced to 23 percent because of a problem with the main
On June 15, reactor power was reduced to 23 percent because of a problem with the main
turbine bypass valves. The reactor was returned to 100 percent power on June 18. The
turbine bypass valves. The reactor was returned to 100 percent power on June 18. The
reactor remained at 100 percent power for the remainder of the inspection period, with the
reactor remained at 100 percent power for the remainder of the inspection period, with the
exception of regularly scheduled power reductions for control rod pattern adjustments and
exception of regularly scheduled power reductions for control rod pattern adjustments and
turbine testing.
turbine testing.
1.     REACTOR SAFETY
1.
        Cornerstones: Initiating Events, Mitigating Systems, Barrier Integrity, Emergency
REACTOR SAFETY
        Preparedness
Cornerstones: Initiating Events, Mitigating Systems, Barrier Integrity, Emergency
1R01 Adverse Weather Protection
Preparedness
  a.   Inspection Scope
1R01
        Hurricane Season Preparations
Adverse Weather Protection
        During the week of June 12, 2006, the inspectors completed a review of the licensee's
    a.
        readiness for seasonal susceptibilities involving high winds at the beginning of hurricane
Inspection Scope
        season. The inspectors reviewed Procedure ENS-EP-302, Severe Weather
Hurricane Season Preparations
        Response, Revision 4. The inspectors: (1) reviewed plant procedures, the Updated
During the week of June 12, 2006, the inspectors completed a review of the licensee's
        Safety Analysis Report (USAR), and Technical Specifications (TS) to verify that operator
readiness for seasonal susceptibilities involving high winds at the beginning of hurricane
        actions defined in adverse weather procedures maintained the readiness of essential
season. The inspectors reviewed Procedure ENS-EP-302, Severe Weather
        systems; (2) walked down portions of the protected area to verify that hurricane season
Response, Revision 4. The inspectors: (1) reviewed plant procedures, the Updated
        preparations were sufficient to support operability of essential systems, including the
Safety Analysis Report (USAR), and Technical Specifications (TS) to verify that operator
        ability to perform safe shutdown functions; (3) evaluated operator staffing levels to verify
actions defined in adverse weather procedures maintained the readiness of essential
        the licensee could maintain the readiness of essential systems required by plant
systems; (2) walked down portions of the protected area to verify that hurricane season
        procedures; and (4) reviewed the corrective action program (CAP) to determine if the
preparations were sufficient to support operability of essential systems, including the
        licensee identified and corrected problems related to adverse weather conditions.
ability to perform safe shutdown functions; (3) evaluated operator staffing levels to verify
        The inspectors completed one inspection sample.
the licensee could maintain the readiness of essential systems required by plant
  b.   Findings
procedures; and (4) reviewed the corrective action program (CAP) to determine if the
        No findings of significance were identified.
licensee identified and corrected problems related to adverse weather conditions.
                                                -6-                                    Enclosure
The inspectors completed one inspection sample.
    b.
Findings
No findings of significance were identified.


1R04 Equipment Alignment
Enclosure
Partial System Walkdowns
-7-
  a.   Inspection Scope
1R04
      The inspectors: (1) walked down portions of the three risk important systems listed
Equipment Alignment
      below and reviewed system operating procedures (SOPs), piping and instrument
  Partial System Walkdowns
      diagrams, and other documents to verify that critical portions of the selected systems
    a.
      were correctly aligned; and (2) compared deficiencies identified during the walkdown to
Inspection Scope
      the licensee's USAR and CAP to verify problems were being identified and corrected.
The inspectors: (1) walked down portions of the three risk important systems listed
      *       Alternate decay heat removal system, which was the backup to the inservice
below and reviewed system operating procedures (SOPs), piping and instrument
                shutdown cooling system during refueling operations, on May 2, 2006
diagrams, and other documents to verify that critical portions of the selected systems
      *       Reactor core isolation cooling system, while the high pressure core spray diesel
were correctly aligned; and (2) compared deficiencies identified during the walkdown to
                was out of service for maintenance, on June 12, 2006
the licensee's USAR and CAP to verify problems were being identified and corrected.  
      *       Division I emergency diesel generator (EDG), while Division II EDG was out of
*
                service for planned maintenance, on June 21, 2006
Alternate decay heat removal system, which was the backup to the inservice
      Documents reviewed by the inspectors included:
shutdown cooling system during refueling operations, on May 2, 2006
      *       SOP-0140, Suppression Pool Cleanup and Alternate Decay Heat Removal,
*
                Revision 16
Reactor core isolation cooling system, while the high pressure core spray diesel
      *       SOP-0035, Reactor Core Isolation Cooling System, Revision 8A
was out of service for maintenance, on June 12, 2006
      *       SOP-0053, Standby Diesel Generator and Auxiliaries, Revision 44A
*
      The inspectors completed three inspection samples.
Division I emergency diesel generator (EDG), while Division II EDG was out of
  h.   Findings
service for planned maintenance, on June 21, 2006  
      No findings of significance were identified.
Documents reviewed by the inspectors included:
1R05 Fire Protection
*
  b.   Inspection Scope
SOP-0140, Suppression Pool Cleanup and Alternate Decay Heat Removal,
      The inspectors walked down the six plant areas listed below to assess the material
Revision 16
      condition of active and passive fire protection features and their operational lineup and
*
      readiness. The inspectors: (1) verified that transient combustibles were controlled in
SOP-0035, Reactor Core Isolation Cooling System, Revision 8A
      accordance with plant procedures; (2) observed the condition of fire detection devices to
*
      verify they remained functional; (3) observed fire suppression systems to verify they
SOP-0053, Standby Diesel Generator and Auxiliaries, Revision 44A
      remained functional and that access to manual actuators was unobstructed; (4) verified
The inspectors completed three inspection samples.
      that fire extinguishers and hose stations were provided at their designated locations and
    h.
                                                -7-                                      Enclosure
Findings
No findings of significance were identified.
1R05
Fire Protection
    b.
Inspection Scope
The inspectors walked down the six plant areas listed below to assess the material
condition of active and passive fire protection features and their operational lineup and
readiness. The inspectors: (1) verified that transient combustibles were controlled in
accordance with plant procedures; (2) observed the condition of fire detection devices to
verify they remained functional; (3) observed fire suppression systems to verify they
remained functional and that access to manual actuators was unobstructed; (4) verified
that fire extinguishers and hose stations were provided at their designated locations and


    that they were in a satisfactory condition; (5) verified that passive fire protection features
Enclosure
    (electrical raceway barriers, fire doors, fire dampers, steel fire proofing, penetration
-8-
    seals, and oil collection systems) were in a satisfactory material condition; (6) verified
that they were in a satisfactory condition; (5) verified that passive fire protection features
    that adequate compensatory measures were established for degraded or inoperable fire
(electrical raceway barriers, fire doors, fire dampers, steel fire proofing, penetration
    protection features and that the compensatory measures were commensurate with the
seals, and oil collection systems) were in a satisfactory material condition; (6) verified
    significance of the deficiency; and (7) reviewed the CAP to determine if the licensee
that adequate compensatory measures were established for degraded or inoperable fire
    identified and corrected fire protection problems.
protection features and that the compensatory measures were commensurate with the
    *       Auxiliary building piping Tunnel D, Fire Area AB-7, on May 9, 2006
significance of the deficiency; and (7) reviewed the CAP to determine if the licensee
    *       Low pressure core spray pump room, Fire Area AB-6/Z-1, on May 9, 2006
identified and corrected fire protection problems.  
    *       High pressure core spray pump room, Fire Area AB-2/Z-1, on May 9, 2006
*
    *       Control building standby switchgear Room 1A, Fire Area C-15, on June 22, 2006
Auxiliary building piping Tunnel D, Fire Area AB-7, on May 9, 2006
    *       Control building safety related cable tray area and stairway Number 3, Fire Area
*
              C-16 and C-29, on June 22, 2006
Low pressure core spray pump room, Fire Area AB-6/Z-1, on May 9, 2006
    *       Division I EDG control and diesel engine rooms, Fire Area DG-6/Z-1, on June 22,
*
              2006
High pressure core spray pump room, Fire Area AB-2/Z-1, on May 9, 2006
    Documents reviewed by the inspectors included:
*
    *       Pre-Fire Plan/Strategy Book
Control building standby switchgear Room 1A, Fire Area C-15, on June 22, 2006
    *       USAR Section 9A.2, Fire Hazards Analysis, Revision 10
*
    *       River Bend Station postfire safe shutdown analysis
Control building safety related cable tray area and stairway Number 3, Fire Area
    *       RBNP-038, Site Fire Protection Program, Revision 6B
C-16 and C-29, on June 22, 2006
    The inspectors completed six inspection samples.
*
  b. Findings
Division I EDG control and diesel engine rooms, Fire Area DG-6/Z-1, on June 22,
    No findings of significance were identified.
2006
1R08 Inservice Inspection Activities
Documents reviewed by the inspectors included:
  a. Inspection Scope
*
    The inspector witnessed the performance of 12 volumetric (ultrasonic) and four surface
Pre-Fire Plan/Strategy Book
    (liquid penetrant) examinations. The sample of nondestructive examination (NDE)
*
    activities is listed in the attachment.
USAR Section 9A.2, Fire Hazards Analysis, Revision 10
    For each of the NDE activities reviewed, the inspector verified that the examinations
*
    were performed in accordance with American Society of Mechanical Engineers (ASME)
River Bend Station postfire safe shutdown analysis
    Code requirements.
*
                                              -8-                                      Enclosure
RBNP-038, Site Fire Protection Program, Revision 6B
The inspectors completed six inspection samples.
    b.
Findings
No findings of significance were identified.
1R08
Inservice Inspection Activities
    a.
Inspection Scope
The inspector witnessed the performance of 12 volumetric (ultrasonic) and four surface
(liquid penetrant) examinations. The sample of nondestructive examination (NDE)
activities is listed in the attachment.  
For each of the NDE activities reviewed, the inspector verified that the examinations
were performed in accordance with American Society of Mechanical Engineers (ASME)
Code requirements.


    During the review of each examination, the inspector verified that appropriate NDE
Enclosure
    procedures were used, that examinations and conditions were as specified in the
-9-
    procedure, and that test instrumentation or equipment was properly calibrated and within
During the review of each examination, the inspector verified that appropriate NDE
    the allowable calibration period. The inspector also reviewed documentation to verify
procedures were used, that examinations and conditions were as specified in the
    that indications revealed by the examinations were dispositioned in accordance with the
procedure, and that test instrumentation or equipment was properly calibrated and within
    ASME Code specified acceptance standards.
the allowable calibration period. The inspector also reviewed documentation to verify
    The inspector verified the certifications of the NDE personnel observed performing
that indications revealed by the examinations were dispositioned in accordance with the
    examinations or identified during review of completed examination packages.
ASME Code specified acceptance standards.
    The inspection procedure requires review of one or two examinations from the previous
The inspector verified the certifications of the NDE personnel observed performing
    outage with recordable indications that were accepted for continued service to ensure
examinations or identified during review of completed examination packages.
    that the disposition was done in accordance with the ASME Code. There were no
The inspection procedure requires review of one or two examinations from the previous
    recordable indications that required evaluation during the last outage.
outage with recordable indications that were accepted for continued service to ensure
    If the licensee completed welding on the pressure boundary for Class 1 or 2 systems
that the disposition was done in accordance with the ASME Code. There were no
    since the beginning of the previous outage, the procedure requires verification that
recordable indications that required evaluation during the last outage.
    acceptance and preservice examinations were done in accordance with the ASME Code
If the licensee completed welding on the pressure boundary for Class 1 or 2 systems
    for one to three welds. There were no welds available for review.
since the beginning of the previous outage, the procedure requires verification that
    The procedure also requires verification that one or two ASME Code Section XI repairs
acceptance and preservice examinations were done in accordance with the ASME Code
    or replacements meet code requirements. There were no code repairs or replacements
for one to three welds. There were no welds available for review.
    available at the time of this inspection.
The procedure also requires verification that one or two ASME Code Section XI repairs
    The inspectors completed 16 inspection samples.
or replacements meet code requirements. There were no code repairs or replacements
  b. Findings
available at the time of this inspection.
    No findings of significance were identified.
The inspectors completed 16 inspection samples.
1R11 Licensed Operator Requalification Program
    b.
  a. Inspection Scope
Findings
    On June 13, 2006, the inspectors observed testing and training of senior reactor
No findings of significance were identified.
    operators and reactor operators to verify the adequacy of training, to assess operator
1R11
    performance, and to assess the evaluators critique. The training evaluation scenario
Licensed Operator Requalification Program
    observed was RSMS-OPS-422, Loss of Circ Water Pump, Failure of Steam Flow
    a.
    Transmitter and Instrument Air System Leak, Revision 4.
Inspection Scope
    The inspectors completed one inspection sample.
On June 13, 2006, the inspectors observed testing and training of senior reactor
  b. Findings
operators and reactor operators to verify the adequacy of training, to assess operator
    No findings of significance were identified.
performance, and to assess the evaluators critique. The training evaluation scenario
                                              -9-                                  Enclosure
observed was RSMS-OPS-422, Loss of Circ Water Pump, Failure of Steam Flow
Transmitter and Instrument Air System Leak, Revision 4.
The inspectors completed one inspection sample.
    b.
Findings
No findings of significance were identified.


1R12 Maintenance Effectiveness
Enclosure
  a. Inspection Scope
-10-
    The inspectors reviewed the condition reports (CR) listed below which documented
1R12
    equipment problems to: (1) verify the appropriate handling of structure, system, and
Maintenance Effectiveness
    component (SSC) performance or condition problems; (2) verify the appropriate
    a.
    handling of degraded SSC functional performance; (3) evaluate the role of work
Inspection Scope
    practices and common cause problems; and (4) evaluate the handling of SSC issues
The inspectors reviewed the condition reports (CR) listed below which documented
    reviewed under the requirements of the maintenance rule; 10 CFR Part 50, Appendix B;
equipment problems to: (1) verify the appropriate handling of structure, system, and
    and TS.
component (SSC) performance or condition problems; (2) verify the appropriate
    *       CR-RBS-2006-1898, main steam stop Valve B21-MOVF098C leakage, reviewed
handling of degraded SSC functional performance; (3) evaluate the role of work
            on June 2, 2006, and CR-RBS-2004-4338, main steam stop Valve B21-
practices and common cause problems; and (4) evaluate the handling of SSC issues
            MOVF098C high leakage during RFO-11 and -12, reviewed on June 26, 2006.
reviewed under the requirements of the maintenance rule; 10 CFR Part 50, Appendix B;
    *       CR-RBS-2006-2302, primary containment integrity maintenance rule repetitive
and TS.  
            functional failure, reviewed on June 26, 2006.
*
    Documents reviewed by the inspectors included:
CR-RBS-2006-1898, main steam stop Valve B21-MOVF098C leakage, reviewed
    *       NUMARC 93-01, Nuclear Energy Institute Industry (NEI) Guideline for Monitoring
on June 2, 2006, and CR-RBS-2004-4338, main steam stop Valve B21-
            the Effectiveness of Maintenance at Nuclear Power Plants, Revision 2
MOVF098C high leakage during RFO-11 and -12, reviewed on June 26, 2006.
    *       Maintenance rule function list
*
    *       Maintenance rule performance criteria list
CR-RBS-2006-2302, primary containment integrity maintenance rule repetitive
    *       Main steam stop valve maintenance rule performance evaluations
functional failure, reviewed on June 26, 2006.
    The inspectors completed two inspection samples.
Documents reviewed by the inspectors included:
  b. Findings
*
    No findings of significance were identified.
NUMARC 93-01, Nuclear Energy Institute Industry (NEI) Guideline for Monitoring
1R13 Maintenance Risk Assessments and Emergent Work Control
the Effectiveness of Maintenance at Nuclear Power Plants, Revision 2
  a. Inspection Scope
*
  .1 Risk Assessment and Management of Risk
Maintenance rule function list
    The inspectors reviewed the planned work weeks listed below to verify: (1) that the
*
    licensee performed risk assessments when required by 10 CFR 50.65 (a)(4) and
Maintenance rule performance criteria list
    administrative Procedure ADM-096, Risk Management Program Implementation and
*
    On-Line Maintenance Risk Assessment, Revision 4B, prior to changes in plant
Main steam stop valve maintenance rule performance evaluations
    configuration for maintenance activities and plant operations; (2) the accuracy,
The inspectors completed two inspection samples.
    adequacy, and completeness of the information considered in the risk assessment;
    b.
                                            -10-                                  Enclosure
Findings
No findings of significance were identified.
1R13
Maintenance Risk Assessments and Emergent Work Control
    a.
Inspection Scope
    .1
Risk Assessment and Management of Risk
The inspectors reviewed the planned work weeks listed below to verify: (1) that the
licensee performed risk assessments when required by 10 CFR 50.65 (a)(4) and
administrative Procedure ADM-096, Risk Management Program Implementation and
On-Line Maintenance Risk Assessment, Revision 4B, prior to changes in plant
configuration for maintenance activities and plant operations; (2) the accuracy,
adequacy, and completeness of the information considered in the risk assessment;


      (3) that the licensee recognized, and entered as applicable, the appropriate licensee
Enclosure
      established risk category according to the risk assessment results and Procedure ADM-
-11-
      096; and (4) that the licensee identified and corrected problems related to maintenance
(3) that the licensee recognized, and entered as applicable, the appropriate licensee
      risk assessments. Specific work activities evaluated included planned and emergent
established risk category according to the risk assessment results and Procedure ADM-
      work for the weeks of:
096; and (4) that the licensee identified and corrected problems related to maintenance
      *       June 5, 2006, Division I work week and preferred station service Transformer
risk assessments. Specific work activities evaluated included planned and emergent
              RTX-ESR1F cooling oil dehydration
work for the weeks of:
      *       June 19, 2006, planned Division II EDG outage week
*
      *       June 26, 2006, nondivisional work week and potential labor work stoppage
June 5, 2006, Division I work week and preferred station service Transformer
  .2 Emergent Work Control
RTX-ESR1F cooling oil dehydration
      For the two emergent work activities listed below, the inspectors: (1) verified that the
*
      licensee performed actions to minimize the probability of initiating events and
June 19, 2006, planned Division II EDG outage week
      maintained the functional capability of mitigating systems and barrier integrity systems;
*
      (2) verified that emergent work related activities such as troubleshooting, work
June 26, 2006, nondivisional work week and potential labor work stoppage
      planning/scheduling, establishing plant conditions, aligning equipment, tagging,
    .2
      temporary modifications, and equipment restoration did not place the plant in an
Emergent Work Control
      unacceptable configuration; and (3) reviewed the CAP to determine if the licensee
For the two emergent work activities listed below, the inspectors: (1) verified that the
      identified and corrected risk assessment and emergent work control problems.
licensee performed actions to minimize the probability of initiating events and
      *       Preferred station service Transformer RTX-ESR1F sudden pressure relay failure
maintained the functional capability of mitigating systems and barrier integrity systems;
              on May 30, 2006
(2) verified that emergent work related activities such as troubleshooting, work
      *       Main turbine bypass valves inoperable due to hydraulic oil leak on June 2, 2006
planning/scheduling, establishing plant conditions, aligning equipment, tagging,
      The inspectors completed five inspection samples.
temporary modifications, and equipment restoration did not place the plant in an
  c. Findings
unacceptable configuration; and (3) reviewed the CAP to determine if the licensee
      No findings of significance were identified.
identified and corrected risk assessment and emergent work control problems.  
1R14 Operator Performance During Nonroutine Evolutions and Events
*
  a. Inspection Scope
Preferred station service Transformer RTX-ESR1F sudden pressure relay failure
  1. April 4, 2006, Automatic Initiation of Standby Service Water
on May 30, 2006
      The inspectors: (1) reviewed operator logs, plant computer data, and strip charts for the
*
      April 4, 2006, unexpected initiation of Division II standby service water that occurred
Main turbine bypass valves inoperable due to hydraulic oil leak on June 2, 2006
      while swapping the running normal service water pumps to evaluate operator
The inspectors completed five inspection samples.
      performance in coping with the event; (2) verified that operator actions were in
    c.
      accordance with the response required by plant procedures and training; and (3) verified
Findings
      that the licensee identified and implemented appropriate corrective actions associated
No findings of significance were identified.
      with personnel performance problems that occurred during the transient. In addition, the
1R14
                                              -11-                                    Enclosure
Operator Performance During Nonroutine Evolutions and Events
    a.
Inspection Scope
    1.
April 4, 2006, Automatic Initiation of Standby Service Water
The inspectors: (1) reviewed operator logs, plant computer data, and strip charts for the
April 4, 2006, unexpected initiation of Division II standby service water that occurred
while swapping the running normal service water pumps to evaluate operator
performance in coping with the event; (2) verified that operator actions were in
accordance with the response required by plant procedures and training; and (3) verified
that the licensee identified and implemented appropriate corrective actions associated
with personnel performance problems that occurred during the transient. In addition, the


      inspectors reviewed CR-RBS-2006-01257, which documented the procedural problems
Enclosure
      that led to the event and reviewed the following procedures used by the operators:
-12-
      *       AOP-53, Initiation of Standby Service Water With Normal Service Water
inspectors reviewed CR-RBS-2006-01257, which documented the procedural problems
              Running, Revision 8
that led to the event and reviewed the following procedures used by the operators:
      *       SOP-42, Standby Service Water System, Revision 25
*
      *       SOP-66, Control Building HVAC Chilled Water System, Revision 33B
AOP-53, Initiation of Standby Service Water With Normal Service Water
  2. April 15, 2006, Reactor Scram
Running, Revision 8
      The inspectors: (1) reviewed operator logs, plant computer data, and strip charts for the
*
      April 15, 2006, unexpected reactor recirculation pump downshift and subsequent reactor
SOP-42, Standby Service Water System, Revision 25
      scram to evaluate operator performance in coping with the event; (2) verified that
*
      operator actions were in accordance with the response required by plant procedures
SOP-66, Control Building HVAC Chilled Water System, Revision 33B
      and training; and (3) verified that the licensee identified and implemented appropriate
    2.
      corrective actions associated with personnel performance problems that occurred during
April 15, 2006, Reactor Scram
      the transient. In addition the inspectors reviewed the postscram report documented in
The inspectors: (1) reviewed operator logs, plant computer data, and strip charts for the
      Procedure GOP-003, Scram Recovery, Revision 16A, and observed the onsite safety
April 15, 2006, unexpected reactor recirculation pump downshift and subsequent reactor
      review committee review of the postscram report.
scram to evaluate operator performance in coping with the event; (2) verified that
      The inspectors completed two inspection samples.
operator actions were in accordance with the response required by plant procedures
  e. Findings
and training; and (3) verified that the licensee identified and implemented appropriate
      No findings of significance were identified.
corrective actions associated with personnel performance problems that occurred during
1R15 Operability Evaluations
the transient. In addition the inspectors reviewed the postscram report documented in
  a. Inspection Scope
Procedure GOP-003, Scram Recovery, Revision 16A, and observed the onsite safety
      For the operability evaluations associated with the documents listed below, the
review committee review of the postscram report.
      inspectors: (1) reviewed plants status documents such as operator shift logs, emergent
The inspectors completed two inspection samples.
      work documentation, deferred modifications, and standing orders, to determine if an
    e.
      operability evaluation was warranted for degraded components; (2) referred to the
Findings
      USAR and design basis documents to review the technical adequacy of licensee
No findings of significance were identified.
      operability evaluations; (3) evaluated compensatory measures associated with
1R15
      operability evaluations; (4) determined degraded component impact on any TS; (5) used
Operability Evaluations
      the significance determination process to evaluate the risk significance of degraded or
    a.
      inoperable equipment; and (6) verified that the licensee identified and implemented
Inspection Scope
      appropriate corrective actions associated with degraded components.
For the operability evaluations associated with the documents listed below, the
      *       CR-RBS-2006-01207 and -01215, Primary containment purge exhaust line fails
inspectors: (1) reviewed plants status documents such as operator shift logs, emergent
              to meet leak rate acceptance criteria, reviewed during the week of April 3, 2006
work documentation, deferred modifications, and standing orders, to determine if an
                                                -12-                                Enclosure
operability evaluation was warranted for degraded components; (2) referred to the
USAR and design basis documents to review the technical adequacy of licensee
operability evaluations; (3) evaluated compensatory measures associated with
operability evaluations; (4) determined degraded component impact on any TS; (5) used
the significance determination process to evaluate the risk significance of degraded or
inoperable equipment; and (6) verified that the licensee identified and implemented
appropriate corrective actions associated with degraded components.  
*
CR-RBS-2006-01207 and -01215, Primary containment purge exhaust line fails
to meet leak rate acceptance criteria, reviewed during the week of April 3, 2006


  *       CR-RBS-2005-02805, Inserted control Rod 24-29 control blade lifetime
Enclosure
          calculation revised for extended operating cycle, reviewed during the week of
-13-
          April 17, 2006
*
  *       Work Request (WR) 76625, NNS-ACB23 control power light out, suspect bad
CR-RBS-2005-02805, Inserted control Rod 24-29 control blade lifetime
          socket, reviewed during the week of May 29, 2006
calculation revised for extended operating cycle, reviewed during the week of
  *       TS-LCO-06-0711, Division II EDG Generator Output Breaker charging springs
April 17, 2006
          did not charge during tagout restoration, reviewed on June 23, 2006
*
  *       CR-RBS-2006-01257, Division II standby service water start on low service water
Work Request (WR) 76625, NNS-ACB23 control power light out, suspect bad
          pressure, reviewed on June 28, 2006
socket, reviewed during the week of May 29, 2006
  *       CR-RBS-2006-02632, turbine bypass valves hydraulic oil leak, reviewed on
*
          June 28, 2006
TS-LCO-06-0711, Division II EDG Generator Output Breaker charging springs
  Other documents reviewed by the inspectors are listed in the attachment.
did not charge during tagout restoration, reviewed on June 23, 2006
  The inspectors completed six inspection samples.
*
b. Findings
CR-RBS-2006-01257, Division II standby service water start on low service water
  Introduction: The inspectors reviewed a self-revealing noncited violation (NCV) of
pressure, reviewed on June 28, 2006
  10 CFR Part 50, Appendix B, Criterion XVI, "Corrective Action," involving the failure of
*
  the licensee to identify that the normal supply breaker to the Division III 4.16 kV
CR-RBS-2006-02632, turbine bypass valves hydraulic oil leak, reviewed on
  engineered safety features (ESF) bus was not properly racked in following maintenance.
June 28, 2006
  Description: Following the completion of planned maintenance on Switchgear NNS-
Other documents reviewed by the inspectors are listed in the attachment.
  SWG1A on April 29, 2006, operators were assigned to clear equipment tags and restore
The inspectors completed six inspection samples.
  the system alignment. As part of this task, operators racked in Breaker NNS-ACB23,
    b.
  the normal supply breaker to 4.16 kV Switchgear NNS-SWG1C. No actions, such as
Findings
  cycling the breaker, were required to verify that the breaker was properly racked in.
Introduction: The inspectors reviewed a self-revealing noncited violation (NCV) of
  On May 9, 2006, after noting that the control power light associated with Breaker NNS-
10 CFR Part 50, Appendix B, Criterion XVI, "Corrective Action," involving the failure of
  ACB23 was not lit, operators wrote WR 76625 to repair the light. The WR stated that
the licensee to identify that the normal supply breaker to the Division III 4.16 kV
  the white control power light on Control Room Panel H13-P808 was out with the breaker
engineered safety features (ESF) bus was not properly racked in following maintenance.  
  racked in and the control power fuses installed. The WR also indicated that the
Description: Following the completion of planned maintenance on Switchgear NNS-
  suspected cause was a bad socket and that position Switch 52H had failed in the past to
SWG1A on April 29, 2006, operators were assigned to clear equipment tags and restore
  make up during closure. A work control center senior reactor operator determined that
the system alignment. As part of this task, operators racked in Breaker NNS-ACB23,
  an operability evaluation was not required for the condition described in WR 76625. The
the normal supply breaker to 4.16 kV Switchgear NNS-SWG1C. No actions, such as
  WR was classified 4D, which indicated that it should be scheduled as resources
cycling the breaker, were required to verify that the breaker was properly racked in.
  allowed within the normal 16-week work planning schedule. The inspectors noted the
On May 9, 2006, after noting that the control power light associated with Breaker NNS-
  licensee did not write a CR. The white control power light provides indication that the
ACB23 was not lit, operators wrote WR 76625 to repair the light. The WR stated that
  breaker is functional, specifically, that: (1) there is no electrical fault on the line or load
the white control power light on Control Room Panel H13-P808 was out with the breaker
  side of the breaker, (2) the breaker Lockout button is not depressed on Panel 808, and
racked in and the control power fuses installed. The WR also indicated that the
  (3) the breaker is fully racked into the switchgear. On May 9, 2006, there were no
suspected cause was a bad socket and that position Switch 52H had failed in the past to
  electrical faults on Breaker NNS-ACB23 and the Lockout was reset on Panel 808.
make up during closure. A work control center senior reactor operator determined that
                                            -13-                                        Enclosure
an operability evaluation was not required for the condition described in WR 76625. The
WR was classified 4D, which indicated that it should be scheduled as resources
allowed within the normal 16-week work planning schedule. The inspectors noted the
licensee did not write a CR. The white control power light provides indication that the
breaker is functional, specifically, that: (1) there is no electrical fault on the line or load
side of the breaker, (2) the breaker Lockout button is not depressed on Panel 808, and
(3) the breaker is fully racked into the switchgear. On May 9, 2006, there were no
electrical faults on Breaker NNS-ACB23 and the Lockout was reset on Panel 808.  


Enclosure
-14-
On May 22, 2006, while aligning Switchgear NNS-SWG1C and the Division III 4.16 kV
On May 22, 2006, while aligning Switchgear NNS-SWG1C and the Division III 4.16 kV
ESF bus to the Transformer RSS1 offsite power supply, Breaker NNS-ACB23 failed to
ESF bus to the Transformer RSS1 offsite power supply, Breaker NNS-ACB23 failed to
close. Operators racked the breaker out and in, but the breaker failed to close on the
close. Operators racked the breaker out and in, but the breaker failed to close on the
second attempt. Subsequent troubleshooting identified that the breaker had not been
second attempt. Subsequent troubleshooting identified that the breaker had not been
fully racked in as electricians were able to rotate the racking device one additional turn.
fully racked in as electricians were able to rotate the racking device one additional turn.  
The white light on Panel 808 came on and the breaker was successfully closed. The
The white light on Panel 808 came on and the breaker was successfully closed. The
operators and electricians determined that Breaker NNS-ACB23 had not been not
operators and electricians determined that Breaker NNS-ACB23 had not been not
properly racked in, wrote CR-RBS-2006-02325 and -02337 and initiated WR 77478 to
properly racked in, wrote CR-RBS-2006-02325 and -02337 and initiated WR 77478 to
investigate the problem with racking in Breaker NNS-ACB23.
investigate the problem with racking in Breaker NNS-ACB23.
On May 25, 2006, the inspectors questioned the impact that the failure of the breaker to
On May 25, 2006, the inspectors questioned the impact that the failure of the breaker to
close had on the licensees compliance with TS. Specifically, TS 3.8.1.a requires two
close had on the licensees compliance with TS. Specifically, TS 3.8.1.a requires two
qualified circuits between the offsite transmission network and the onsite Class 1E ac
qualified circuits between the offsite transmission network and the onsite Class 1E ac
electrical power distribution system when the plant is in Modes 1, 2, and 3. On May 12,
electrical power distribution system when the plant is in Modes 1, 2, and 3. On May 12,
the plant was taken from Mode 4 to Mode 2 without two qualified offsite power sources
the plant was taken from Mode 4 to Mode 2 without two qualified offsite power sources
available to the Division III 4.16 kV ESF bus. The licensee wrote CR-RBS-2006-2402
available to the Division III 4.16 kV ESF bus. The licensee wrote CR-RBS-2006-2402
and determined that they did not comply with TS 3.8.1.a when they changed modes on
and determined that they did not comply with TS 3.8.1.a when they changed modes on
May 12. In addition, the Division III 4.16 kV ESF bus was inoperable for a period of
May 12. In addition, the Division III 4.16 kV ESF bus was inoperable for a period of
10 days (May 12-22), which exceeded the allowed outage time of 72 hours specified in
10 days (May 12-22), which exceeded the allowed outage time of 72 hours specified in
TS Condition 3.8.1.A. The licensee also discovered that, on May 14 during the conduct
TS Condition 3.8.1.A. The licensee also discovered that, on May 14 during the conduct
of maintenance on the Division I EDG, with Breaker NNS-ACB23 unable to be closed,
of maintenance on the Division I EDG, with Breaker NNS-ACB23 unable to be closed,
they unknowingly entered TS Condition 3.8.1.d. TS Condition 3.8.1.d states that with
they unknowingly entered TS Condition 3.8.1.d. TS Condition 3.8.1.d states that with
One required offsite circuit inoperable AND on required [E]DG inoperable, restore the
One required offsite circuit inoperable AND on required [E]DG inoperable, restore the
EDG or the offsite power supply to an operable status in 12 hours or place the plant in
EDG or the offsite power supply to an operable status in 12 hours or place the plant in
Mode 3 within the next 12 hours. The Division I EDG was inoperable for 15 hours and
Mode 3 within the next 12 hours. The Division I EDG was inoperable for 15 hours and
15 minutes.
15 minutes.
The inspectors found that the licensees procedures did not require Breaker NNS-
The inspectors found that the licensees procedures did not require Breaker NNS-
ACB23 to be cycled to verify proper operation after it was racked in on April 29.
ACB23 to be cycled to verify proper operation after it was racked in on April 29.  
Procedure OSP-0022, Operations General Administrative Guidelines, Revision 01,
Procedure OSP-0022, Operations General Administrative Guidelines, Revision 01,
step 4.5.5, required that breakers be functionally tested following any activity involving
step 4.5.5, required that breakers be functionally tested following any activity involving
safety related equipment which requires the breaker to be racked out. Because
safety related equipment which requires the breaker to be racked out. Because
Breaker NNS-ACB23 is not classified as a safety-related breaker, it was not required to
Breaker NNS-ACB23 is not classified as a safety-related breaker, it was not required to
be functionally tested after it was racked in on April 29.
be functionally tested after it was racked in on April 29.  
Analysis: The performance deficiency associated with this finding involved the failure of
Analysis: The performance deficiency associated with this finding involved the failure of
operators to identify that Breaker NNS-ACB23 was not functional on April 29, 2006. The
operators to identify that Breaker NNS-ACB23 was not functional on April 29, 2006. The
finding was more than minor because it was associated with the mitigating system
finding was more than minor because it was associated with the mitigating system
cornerstone attribute of configuration control and affected the associated cornerstone
cornerstone attribute of configuration control and affected the associated cornerstone
objective to ensure the availability, reliability, and capability of systems that respond to
objective to ensure the availability, reliability, and capability of systems that respond to
initiating events to prevent undesirable consequences. The Phase 1 worksheets in
initiating events to prevent undesirable consequences. The Phase 1 worksheets in
Manual Chapter (MC) 0609, "Significance Determination Process," were used to
Manual Chapter (MC) 0609, "Significance Determination Process," were used to
conclude that a Phase 2 analysis was required because both the mitigating systems and
conclude that a Phase 2 analysis was required because both the mitigating systems and
the containment barrier cornerstones were affected.
the containment barrier cornerstones were affected.
In accordance with NRC Inspection Manual Chapter 0609, Appendix A, Attachment 1,
In accordance with NRC Inspection Manual Chapter 0609, Appendix A, Attachment 1,
"User Guidance for Determining the Significance of Reactor Inspection Findings for
"User Guidance for Determining the Significance of Reactor Inspection Findings for
At-Power Situations," the inspectors estimated the risk of the subject finding using the
At-Power Situations," the inspectors estimated the risk of the subject finding using the
                                          -14-                                      Enclosure


Risk-Informed Inspection Notebook for River Bend Station, Revision 2. The inspectors
Enclosure
-15-
Risk-Informed Inspection Notebook for River Bend Station, Revision 2. The inspectors
assumed that Division III power was available, but degraded, while Breaker NNS-ACB23
assumed that Division III power was available, but degraded, while Breaker NNS-ACB23
was not properly installed for the 10 days that the plant was in Mode 3 or above, from
was not properly installed for the 10 days that the plant was in Mode 3 or above, from
May 12-22, 2006. Therefore, the exposure window used was 3-30 days. No operator
May 12-22, 2006. Therefore, the exposure window used was 3-30 days. No operator
recovery was credited because on two occasions, operators had proven incapable of
recovery was credited because on two occasions, operators had proven incapable of
properly positioning the breaker, ultimately requiring maintenance technicians to
properly positioning the breaker, ultimately requiring maintenance technicians to
properly install the breaker. Using Manual Chapter 0609, Appendix A, Attachment 2,
properly install the breaker. Using Manual Chapter 0609, Appendix A, Attachment 2,
Rule 2.1, Inspection Finding that Degrades Mitigation Capability and Does Not Reduce
Rule 2.1, Inspection Finding that Degrades Mitigation Capability and Does Not Reduce
Remaining Mitigation Capability Credit to a Value Less Than Full Mitigation Credit, the
Remaining Mitigation Capability Credit to a Value Less Than Full Mitigation Credit, the
Line 669: Line 813:
by a loss of Division III power, including the Division I standby service water loop
by a loss of Division III power, including the Division I standby service water loop
(HPCS, LPI, CHR, HPCS/LC, and REC/SSW), should be quantified, giving full mitigation
(HPCS, LPI, CHR, HPCS/LC, and REC/SSW), should be quantified, giving full mitigation
capability credit to each of these functions. Because the performance deficiency
capability credit to each of these functions. Because the performance deficiency
affected the electric power system, Table 2 of the risk-informed notebook required that
affected the electric power system, Table 2 of the risk-informed notebook required that
all worksheets be evaluated. The resulting dominant sequences are provided in Table 1
all worksheets be evaluated. The resulting dominant sequences are provided in Table 1
below:
below:
                                                              Table 1
Table 1
                                                  Phase 2 Worksheet Results
Phase 2 Worksheet Results
    Initiator       Sequence           IEL                       Mitigating Functions Result
Initiator
    TNSW               5               3                         SSW - REC/SSW         7*
Sequence
                        4               3                       RCIC - HPCS - DEP     9*
IEL
                        1               3                           CHR - LDEP         8
Mitigating Functions
                        2               3                         CHR - SPCFAN         8
Result
    LOOP              4               3                       RCIC - HPCS - DEP     9*
TNSW
                        6               3                 EAC1&2 - HPCS - REC6 - FPW   9*
5
                        8               3                 EAC1&2 - HPCS - SBODG - REC4 9*
3
                        9               3                   EAC1&2 - REC1 - HPCS -RCIC 9*
SSW - REC/SSW
                        1               3                             CHR-LDEP           8
7*
    SORV              2               3                         CHR - SPCFAN         9
4
                        4               3                       RCIC - HPCS - DEP     9*
3
                        2               4                         CHR - SPCFAN         8
RCIC - HPCS - DEP
      LOIA
9*
                        1                4                             CHR-LDEP           9
LOOP
    TPCS               4               2                       RCIC - HPCS - DEP       8
1
    ATWS               1               6                               CHR             9
3
CHR - LDEP
8
2
3
CHR - SPCFAN
8
4
3
RCIC - HPCS - DEP
9*
6
3
EAC1&2 - HPCS - REC6 - FPW  
9*
8
3
EAC1&2 - HPCS - SBODG - REC4  
9*
9
3
EAC1&2 - REC1 - HPCS -RCIC
9*
SORV
1
3
CHR-LDEP
8
2
3
CHR - SPCFAN
9
4
3
RCIC - HPCS - DEP
9*
LOIA
2
4
CHR - SPCFAN
8
1
4
CHR-LDEP
9
TPCS
4
2
RCIC - HPCS - DEP
8
ATWS
1
6
CHR
9
     * Denotes sequences indicated as LERF contributors in the Phase 2 notebook.
     * Denotes sequences indicated as LERF contributors in the Phase 2 notebook.
By application of the counting rule, the internal event risk contribution of this finding to
By application of the counting rule, the internal event risk contribution of this finding to
Line 697: Line 895:
risk significance (WHITE).
risk significance (WHITE).
A senior reactor analyst performed further evaluation of the risk associated with this
A senior reactor analyst performed further evaluation of the risk associated with this
issue (Phase 3/Modified Phase 2). Because the assumptions made during the Phase 2
issue (Phase 3/Modified Phase 2). Because the assumptions made during the Phase 2
estimation process were overly conservative and did not completely represent the actual
estimation process were overly conservative and did not completely represent the actual
exposure time nor the actual affect the performance deficiency had on the availability of
exposure time nor the actual affect the performance deficiency had on the availability of
power to the Division III diesel generator, the senior reactor analyst modified these
power to the Division III diesel generator, the senior reactor analyst modified these
                                                        -15-                              Enclosure


assumptions to more precisely quantify the change in risk. Specifically, the exposure
Enclosure
time was 10 days as opposed to the 30 days used in the risk-informed notebook.
-16-
assumptions to more precisely quantify the change in risk. Specifically, the exposure
time was 10 days as opposed to the 30 days used in the risk-informed notebook.  
Additionally, the Phase 2 evaluation included loss of offsite power initiating events that
Additionally, the Phase 2 evaluation included loss of offsite power initiating events that
were not affected by the performance deficiency because offsite power to Division III
were not affected by the performance deficiency because offsite power to Division III
would in all likelihood be lost during a design basis loss of offsite power. The senior
would in all likelihood be lost during a design basis loss of offsite power. The senior
reactor analyst performed a modified Phase 2 estimation and determined that the
reactor analyst performed a modified Phase 2 estimation and determined that the
internal event risk contribution of the subject finding to the CDF was of very low risk
internal event risk contribution of the subject finding to the CDF was of very low risk
significance (Green). The best estimate value of this probability (CDFINTERNAL) was
significance (Green). The best estimate value of this probability (CDFINTERNAL) was
calculated by the senior reactor analyst to be 1.2 x 10-7. The analyst evaluated the
calculated by the senior reactor analyst to be 1.2 x 10-7. The analyst evaluated the
contribution of external initiating events to the risk and calculated a bounding risk
contribution of external initiating events to the risk and calculated a bounding risk
estimate of 2.9 x 10-7 as the CDF for internal fire events.
estimate of 2.9 x 10-7 as the CDF for internal fire events.
Line 719: Line 918:
Given the independence of each initiating event, the analyst determined that the best
Given the independence of each initiating event, the analyst determined that the best
estimate of the total risk related to the subject performance deficiency was the
estimate of the total risk related to the subject performance deficiency was the
summation of the CDF calculated for both internal and external initiators. Therefore,
summation of the CDF calculated for both internal and external initiators. Therefore,
the best estimate was 4.1 x 10-7. The change in risk related to large early release
the best estimate was 4.1 x 10-7. The change in risk related to large early release
frequency was determined to be below 6.6 x 10-8, corroborating that the finding was of
frequency was determined to be below 6.6 x 10-8, corroborating that the finding was of
very low risk significance. The performance deficiency resulted in a finding that was of
very low risk significance. The performance deficiency resulted in a finding that was of
very low risk significance (Green). The cause of the finding was related to the
very low risk significance (Green). The cause of the finding was related to the
crosscutting aspect of problem identification and resolution in that operators failed to
crosscutting aspect of problem identification and resolution in that operators failed to
identify that Breaker NNS-ACB23 was not properly racked in.
identify that Breaker NNS-ACB23 was not properly racked in.
Enforcement: 10 CFR Part 50, Appendix B, Criterion XVI, Corrective Action, requires, in
Enforcement: 10 CFR Part 50, Appendix B, Criterion XVI, Corrective Action, requires, in
part, that measures be established to assure that conditions adverse to quality are
part, that measures be established to assure that conditions adverse to quality are
promptly identified and corrected. Contrary to this, from April 29 to May 22, 2006, the
promptly identified and corrected. Contrary to this, from April 29 to May 22, 2006, the
licensee failed to identify that Breaker NNS-ACB23, which supplied one of the two
licensee failed to identify that Breaker NNS-ACB23, which supplied one of the two
required offsite power supplies to the Division III 4.16 kV ESF bus, was not properly
required offsite power supplies to the Division III 4.16 kV ESF bus, was not properly
racked in to Switchgear NNS-SWGIC. The root cause involved the licensees lack of
racked in to Switchgear NNS-SWGIC. The root cause involved the licensees lack of
understanding that Breaker NNS-ACB23 was required to be functional to meet
understanding that Breaker NNS-ACB23 was required to be functional to meet
TS 3.8.1.a requirements for two offsite power circuits to the Division III 4.16 kV ESF
TS 3.8.1.a requirements for two offsite power circuits to the Division III 4.16 kV ESF
bus. The corrective actions to restore compliance included: (1) changes to operations
bus. The corrective actions to restore compliance included: (1) changes to operations
section procedures to verify the white control power light, when applicable, after a circuit
section procedures to verify the white control power light, when applicable, after a circuit
breaker is racked in, (2) expansion of the requirement to functionally test safety-related
breaker is racked in, (2) expansion of the requirement to functionally test safety-related
breakers to the nonsafety-related breakers in the TS required offsite power circuits, and
breakers to the nonsafety-related breakers in the TS required offsite power circuits, and
(3) operator lessons learned training on the event and all of its ramifications. Because
(3) operator lessons learned training on the event and all of its ramifications. Because
the finding was of very low safety significance and has been entered into the licensees
the finding was of very low safety significance and has been entered into the licensees
CAP as CR-RBS-2006-02402, this violation is being treated as an NCV consistent with
CAP as CR-RBS-2006-02402, this violation is being treated as an NCV consistent with
Section VI.A of the Enforcement Policy: NCV 05000458/2006003-01, Failure to identify
Section VI.A of the Enforcement Policy: NCV 05000458/2006003-01, Failure to identify
Division III ESF bus supply breaker not racked in.
Division III ESF bus supply breaker not racked in.
                                          -16-                                    Enclosure


1R19 Postmaintenance Testing
Enclosure
  a. Inspection Scope
-17-
    For the five postmaintenance test activities of risk significant systems or components
1R19
    listed below, the inspectors: (1) reviewed the applicable licensing basis and/or design-
Postmaintenance Testing
    basis documents to determine the safety functions; (2) evaluated the safety functions
    a.
    that may have been affected by the maintenance activity; and (3) reviewed the test
Inspection Scope
    procedure to verify that it adequately tested the safety function that may have been
For the five postmaintenance test activities of risk significant systems or components
    affected. The inspectors either witnessed or reviewed test data to verify that
listed below, the inspectors: (1) reviewed the applicable licensing basis and/or design-
    acceptance criteria were met, plant impacts were evaluated, test equipment was
basis documents to determine the safety functions; (2) evaluated the safety functions
    calibrated, procedures were followed, jumpers were properly controlled, the test data
that may have been affected by the maintenance activity; and (3) reviewed the test
    results were complete and accurate, the test equipment was removed, the system was
procedure to verify that it adequately tested the safety function that may have been
    properly re-aligned, and deficiencies during testing were documented. The inspectors
affected. The inspectors either witnessed or reviewed test data to verify that
    also reviewed the CAP to determine if the licensee identified and corrected problems
acceptance criteria were met, plant impacts were evaluated, test equipment was
    related to postmaintenance testing.
calibrated, procedures were followed, jumpers were properly controlled, the test data
    *       Work Order (WO) 50370422, Division II battery cell post seal replacement,
results were complete and accurate, the test equipment was removed, the system was
            reviewed during the week of May 8, 2006
properly re-aligned, and deficiencies during testing were documented. The inspectors
    *       WO 87721, replace control Rods 40-37, 44-41, and 48-25 and 12-25 individual
also reviewed the CAP to determine if the licensee identified and corrected problems
            scram test switches, reviewed May 19, 2006
related to postmaintenance testing.  
    *       WO 69816, low pressure core spray keep fill pump discharge check valve, E21-
*
            VF033 replacement, reviewed during the week of June 19, 2006
Work Order (WO) 50370422, Division II battery cell post seal replacement,
    *       WO 85194, signature testing on high pressure core spray room unit cooler
reviewed during the week of May 8, 2006
            service water outlet valve, SWP-MOV74B, reviewed during the week of June 19,
*
            2006
WO 87721, replace control Rods 40-37, 44-41, and 48-25 and 12-25 individual
    *       WO 90342, Division II EDG generator output Breaker ENS-SWG1B-ACB027
scram test switches, reviewed May 19, 2006
            charging springs failed to charge during tagout restoration, reviewed on June 23,
*
            2006
WO 69816, low pressure core spray keep fill pump discharge check valve, E21-
    The inspectors completed five inspection samples.
VF033 replacement, reviewed during the week of June 19, 2006
  g. Findings
*
    No findings of significance were identified.
WO 85194, signature testing on high pressure core spray room unit cooler
1R20 Refueling and Other Outage Activities
service water outlet valve, SWP-MOV74B, reviewed during the week of June 19,
  a. Inspection Scope
2006
    The inspectors reviewed the following risk important refueling outage activities to verify
*
    defense in depth commensurate with the outage risk control plan and compliance with
WO 90342, Division II EDG generator output Breaker ENS-SWG1B-ACB027
    the TS during RFO-13 from April 23 to May 12, 2006: (1) the risk control plan;
charging springs failed to charge during tagout restoration, reviewed on June 23,
    (2) tagging/clearance activities; (3) reactor coolant system instrumentation; (4) electrical
2006
                                              -17-                                    Enclosure
The inspectors completed five inspection samples.
    g.
Findings
No findings of significance were identified.
1R20
Refueling and Other Outage Activities
    a.
Inspection Scope
The inspectors reviewed the following risk important refueling outage activities to verify
defense in depth commensurate with the outage risk control plan and compliance with
the TS during RFO-13 from April 23 to May 12, 2006: (1) the risk control plan;
(2) tagging/clearance activities; (3) reactor coolant system instrumentation; (4) electrical


  power; (5) decay heat removal; (6) spent fuel pool cooling; (7) inventory control;
Enclosure
  (8) reactivity control; (9) containment closure; (10) reduced inventory conditions;
-18-
  (11) refueling activities; (12) heatup and cooldown activities; (13) restart activities; and
power; (5) decay heat removal; (6) spent fuel pool cooling; (7) inventory control;
  (14) licensee identification and implementation of appropriate corrective actions
(8) reactivity control; (9) containment closure; (10) reduced inventory conditions;
  associated with RFO activities. The inspectors' containment inspections included
(11) refueling activities; (12) heatup and cooldown activities; (13) restart activities; and
  observations of the containment sump for damage and debris, and supports, braces,
(14) licensee identification and implementation of appropriate corrective actions
  and snubbers for evidence of excessive stress, water hammer, or aging. Specific
associated with RFO activities. The inspectors' containment inspections included
  outage activities observed and reviewed included:
observations of the containment sump for damage and debris, and supports, braces,
  *       Outage risk assessment team (ORAT) report to onsite safety review committee
and snubbers for evidence of excessive stress, water hammer, or aging. Specific
  *       Reactor shutdown, cooldown, and vessel disassembly
outage activities observed and reviewed included:
  *       Refueling operations, fuel sipping, and off loaded fuel inspections
*
  *       Daily/shiftly shutdown operations protection plan assessments
Outage risk assessment team (ORAT) report to onsite safety review committee
  *       Shutdown postscram report to onsite safety review committee
*
  *       Reactor recirculation pump trip logic modification installation and testing
Reactor shutdown, cooldown, and vessel disassembly
  *       Main steam line local leak rate testing
*
  *       Transformer RSS1 offsite power line equipment inspection and upgrade
Refueling operations, fuel sipping, and off loaded fuel inspections
  *       Division II to Division I protected division swap
*
  *       Infrequently performed test or evolution briefings for:
Daily/shiftly shutdown operations protection plan assessments
          - Divisional loss of offsite power/loss of coolant accident testing
*
          - Concurrent control rod mechanism and blade changeout
Shutdown postscram report to onsite safety review committee
          - Reactor vessel pressure test and scram time testing
*
          - Reactor startup, heatup, and power ascension
Reactor recirculation pump trip logic modification installation and testing
          - Onsite safety review committee meeting to recommend startup
*
          - Drywell 900 psi walkdown (after shutdown and during startup)
Main steam line local leak rate testing
  Documents reviewed by the inspectors are listed in the attachment.
*
  The inspectors completed one inspection sample.
Transformer RSS1 offsite power line equipment inspection and upgrade
b. Findings
*
  Introduction: An NRC identified NCV of 10 CFR 50.65, Maintenance Rule,
Division II to Division I protected division swap
  Section (a)(4) was identified for the failure of the licensee to provide prescribed
*
  compensatory measures for the highest shutdown risk condition during RFO-13.
Infrequently performed test or evolution briefings for:
  Specifically, the preoutage risk assessment recommended that two WOs be in place for
- Divisional loss of offsite power/loss of coolant accident testing
  maintenance electricians to provide power to one spent fuel pool cooling pump in the
- Concurrent control rod mechanism and blade changeout
  event of problems with the running pump during periods of safety-related electrical bus
- Reactor vessel pressure test and scram time testing
  maintenance. The inspectors found that the WOs were not in place before entering
- Reactor startup, heatup, and power ascension
  shutdown risk condition Orange on April 26, 2006, during the Division II ESF bus testing,
- Onsite safety review committee meeting to recommend startup
  and on May 3, 2006, during the Division I ESF bus outage.
- Drywell 900 psi walkdown (after shutdown and during startup)
  Description: The inspectors observed the onsite safety review committee meeting to
Documents reviewed by the inspectors are listed in the attachment.
  discuss and approve the ORAT report for RFO-13. The report noted two Orange
The inspectors completed one inspection sample.
  shutdown risk conditions for spent fuel pool cooling (SFC). Only one SFC pump would
    b.
  be available after the beginning of core offload: (1) during the Division II ESF bus
Findings
  testing with the SFC-P1B breaker racked out, and (2) during the Division I ESF bus
Introduction: An NRC identified NCV of 10 CFR 50.65, Maintenance Rule,
  outage when SFC-P1A was without power. As a result of the ORAT review of
Section (a)(4) was identified for the failure of the licensee to provide prescribed
                                            -18-                                    Enclosure
compensatory measures for the highest shutdown risk condition during RFO-13.  
Specifically, the preoutage risk assessment recommended that two WOs be in place for
maintenance electricians to provide power to one spent fuel pool cooling pump in the
event of problems with the running pump during periods of safety-related electrical bus
maintenance. The inspectors found that the WOs were not in place before entering
shutdown risk condition Orange on April 26, 2006, during the Division II ESF bus testing,
and on May 3, 2006, during the Division I ESF bus outage.
Description: The inspectors observed the onsite safety review committee meeting to
discuss and approve the ORAT report for RFO-13. The report noted two Orange
shutdown risk conditions for spent fuel pool cooling (SFC). Only one SFC pump would
be available after the beginning of core offload: (1) during the Division II ESF bus
testing with the SFC-P1B breaker racked out, and (2) during the Division I ESF bus
outage when SFC-P1A was without power. As a result of the ORAT review of


Enclosure
-19-
Procedure AOP-0051, Loss of Decay Heat Removal, Revision 17, they recommended
Procedure AOP-0051, Loss of Decay Heat Removal, Revision 17, they recommended
that the planned maintenance optimization group develop WOs for maintenance
that the planned maintenance optimization group develop WOs for maintenance
Line 831: Line 1,054:
deenergized SFC pump in the event of a failure of the running pump.
deenergized SFC pump in the event of a failure of the running pump.
In addition, Procedure OSP-0037, Shutdown Operations Protection Plan, Revision 16,
In addition, Procedure OSP-0037, Shutdown Operations Protection Plan, Revision 16,
Section 4.7, Fuel Pool Cooling, required that: (1) if work was required on SFC during
Section 4.7, Fuel Pool Cooling, required that: (1) if work was required on SFC during
the outage, then it should be done as early as possible in the outage and not after fuel
the outage, then it should be done as early as possible in the outage and not after fuel
offload (when heat load is the highest); and (2) if work was required after fuel offload,
offload (when heat load is the highest); and (2) if work was required after fuel offload,
then a contingency plan shall be in place prior to removing the system from service.
then a contingency plan shall be in place prior to removing the system from service.  
The inspectors determined that this requirement applied to deenergizing an SFC pump
The inspectors determined that this requirement applied to deenergizing an SFC pump
for electrical bus maintenance.
for electrical bus maintenance.
On May 3, 2006, during the Division I ESF bus outage, the inspectors asked the
On May 3, 2006, during the Division I ESF bus outage, the inspectors asked the
operations shift manager if the required WO was available to provide alternate power to
operations shift manager if the required WO was available to provide alternate power to
SFC-P1A in the event that the running SFC-P1B failed. He stated that he assumed that
SFC-P1A in the event that the running SFC-P1B failed. He stated that he assumed that
the WO was written and that he would check. The inspectors then requested a copy of
the WO was written and that he would check. The inspectors then requested a copy of
the WO and a senior work planner reported that the WO was not available since it was
the WO and a senior work planner reported that the WO was not available since it was
not yet approved for use in the electronic work planning program. Following discussions
not yet approved for use in the electronic work planning program. Following discussions
with operators in the work management center, the licensee immediately took actions to
with operators in the work management center, the licensee immediately took actions to
ensure that both WOs were processed and made ready for use.
ensure that both WOs were processed and made ready for use.
The inspectors reviewed AOP-0051, Attachment 1, Spent Fuel Pool Curves, and
The inspectors reviewed AOP-0051, Attachment 1, Spent Fuel Pool Curves, and
determined that the approximate time to boil for the spent fuel pool at that time with
determined that the approximate time to boil for the spent fuel pool at that time with
offload fuel in the pool was approximately 8 hours. Based on that data and the time
offload fuel in the pool was approximately 8 hours. Based on that data and the time
needed to generate the WOs, the inspectors determined that there was adequate time
needed to generate the WOs, the inspectors determined that there was adequate time
for the licensee to connect an alternate power supply to the SFC pumps before the
for the licensee to connect an alternate power supply to the SFC pumps before the
spent fuel pool water started to boil if there was a failure of the running pump.
spent fuel pool water started to boil if there was a failure of the running pump.
Analysis: The performance deficiency associated with this finding involved the failure to
Analysis: The performance deficiency associated with this finding involved the failure to
establish prescribed compensatory measures for the highest outage risk condition
establish prescribed compensatory measures for the highest outage risk condition
during RFO-13 as required by the shutdown operations protection plan. The finding was
during RFO-13 as required by the shutdown operations protection plan. The finding was
more than minor because the licensee failed to implement prescribed compensatory
more than minor because the licensee failed to implement prescribed compensatory
measures and failed to effectively manage those measures. The finding affected the
measures and failed to effectively manage those measures. The finding affected the
mitigating system cornerstone because of the increased risk of a sustained loss of SFC
mitigating system cornerstone because of the increased risk of a sustained loss of SFC
during core offloading operations. The finding could not be evaluated using the
during core offloading operations. The finding could not be evaluated using the
significance determination process; therefore, the finding was reviewed by regional
significance determination process; therefore, the finding was reviewed by regional
management and determined to be of very low safety significance. Factors that were
management and determined to be of very low safety significance. Factors that were
considered included: (1) electrical maintenance technicians had previously performed
considered included: (1) electrical maintenance technicians had previously performed
the task of providing alternate power to an SFC pump, (2) the necessary equipment was
the task of providing alternate power to an SFC pump, (2) the necessary equipment was
staged as part of the abnormal operating procedure for loss of decay heat removal, and
staged as part of the abnormal operating procedure for loss of decay heat removal, and
(3) the relatively long time to boil of the spent fuel storage pool at that time during the
(3) the relatively long time to boil of the spent fuel storage pool at that time during the
refueling outage. The cause of the finding was related to the crosscutting aspect of
refueling outage. The cause of the finding was related to the crosscutting aspect of
human performance because the licensees planned maintenance activities and the
human performance because the licensees planned maintenance activities and the
predetermined increase in outage risk was not effectively managed by prescribed
predetermined increase in outage risk was not effectively managed by prescribed
compensatory measures.
compensatory measures.
                                          -19-                                    Enclosure


    Enforcement: 10 CFR 50.65(a)(4) requires, in part, that before performing maintenance
Enclosure
    activities, the licensee shall assess and manage the increase in risk that may result from
-20-
    the proposed maintenance activities. Contrary to this, the licensee failed to properly
Enforcement: 10 CFR 50.65(a)(4) requires, in part, that before performing maintenance
    manage the highest outage risk condition of RFO-13. On April 26, 2006, the plant
activities, the licensee shall assess and manage the increase in risk that may result from
    entered an Orange outage risk condition for SFC during core offload, when SFC-P1B
the proposed maintenance activities. Contrary to this, the licensee failed to properly
    was deenergized for Division II ESF bus testing. On May 3, 2006, the plant entered an
manage the highest outage risk condition of RFO-13. On April 26, 2006, the plant
    Orange outage risk condition for SFC during core offload, when SFC-P1A was
entered an Orange outage risk condition for SFC during core offload, when SFC-P1B
    deenergized for a Division I ESF bus outage. WOs were not written and ready for use
was deenergized for Division II ESF bus testing. On May 3, 2006, the plant entered an
    to have electricians provide alternate power to an SFC pump in the event the running
Orange outage risk condition for SFC during core offload, when SFC-P1A was
    pump failed. The root cause involved the failure of the licensee to ensure that the WO
deenergized for a Division I ESF bus outage. WOs were not written and ready for use
    was in place before the plant entered the Orange shutdown risk condition. Corrective
to have electricians provide alternate power to an SFC pump in the event the running
    action was taken to process the WOs for immediate use. Because the finding was of
pump failed. The root cause involved the failure of the licensee to ensure that the WO
    very low safety significance and was entered into the licensees CAP as CR-RBS-2006-
was in place before the plant entered the Orange shutdown risk condition. Corrective
    01937, this violation is being treated as an NCV consistent with Section VI.A of the
action was taken to process the WOs for immediate use. Because the finding was of
    Enforcement Policy: NCV 05000458/2006003-02, "Failure to adequately manage an
very low safety significance and was entered into the licensees CAP as CR-RBS-2006-
    increase in plant risk."
01937, this violation is being treated as an NCV consistent with Section VI.A of the
1R22 Surveillance Testing
Enforcement Policy: NCV 05000458/2006003-02, "Failure to adequately manage an
  a. Inspection Scope
increase in plant risk."  
    The inspectors reviewed the USAR, procedure requirements, and TS to ensure that the
1R22
    six surveillance activities listed below demonstrated that the SSCs tested were capable
Surveillance Testing
    of performing their intended safety functions. The inspectors either witnessed or
    a.
    reviewed test data to verify that the following significant surveillance test attributes were
Inspection Scope
    adequate: (1) preconditioning; (2) evaluation of testing impact on the plant;
The inspectors reviewed the USAR, procedure requirements, and TS to ensure that the
    (3) acceptance criteria; (4) test equipment; (5) procedures; (6) jumper/lifted lead
six surveillance activities listed below demonstrated that the SSCs tested were capable
    controls; (7) test data; (8) testing frequency and method demonstrated TS operability;
of performing their intended safety functions. The inspectors either witnessed or
    (9) test equipment removal; (10) restoration of plant systems; (11) fulfillment of ASME
reviewed test data to verify that the following significant surveillance test attributes were
    Code requirements; (12) updating of performance indicator (PI) data; (13) engineering
adequate: (1) preconditioning; (2) evaluation of testing impact on the plant;
    evaluations, root causes, and bases for returning tested SSCs not meeting the test
(3) acceptance criteria; (4) test equipment; (5) procedures; (6) jumper/lifted lead
    acceptance criteria were correct; (14) reference setting data; and (15) annunciator and
controls; (7) test data; (8) testing frequency and method demonstrated TS operability;
    alarm setpoints. The inspectors also verified that the licensee identified and
(9) test equipment removal; (10) restoration of plant systems; (11) fulfillment of ASME
    implemented any needed corrective actions associated with the surveillance testing.
Code requirements; (12) updating of performance indicator (PI) data; (13) engineering
    *       STP-208-3601, "A Main Steam Line MSIVs and Outboard Drain Valve Leak
evaluations, root causes, and bases for returning tested SSCs not meeting the test
              Rate Test and Inboard MSIV Inleakage Test," Revision 6, performed on May 2,
acceptance criteria were correct; (14) reference setting data; and (15) annunciator and
              2006
alarm setpoints. The inspectors also verified that the licensee identified and
    *       STP-305-1606, [Division I Battery] ENB-BAT1A Service Discharge Test,
implemented any needed corrective actions associated with the surveillance testing.  
              Revision 17, performed on May 6, 2006
*
    *       STP-050-3601, Shutdown Margin Demonstration, Revision 27, performed on
STP-208-3601, "A Main Steam Line MSIVs and Outboard Drain Valve Leak
              May 12, 2006
Rate Test and Inboard MSIV Inleakage Test," Revision 6, performed on May 2,
    *       STP-000-0102, Power Distribution Alignment Check, Revision 5, performed on
2006
              May 14 and 15, 2006
*
                                              -20-                                      Enclosure
STP-305-1606, [Division I Battery] ENB-BAT1A Service Discharge Test,
Revision 17, performed on May 6, 2006
*
STP-050-3601, Shutdown Margin Demonstration, Revision 27, performed on
May 12, 2006
*
STP-000-0102, Power Distribution Alignment Check, Revision 5, performed on
May 14 and 15, 2006


  *       STP-508-4543, Turbine First Stage Pressure Channel Functional Test,
Enclosure
            Revision 7, performed on June 4, 2006
-21-
  *       Reactor coolant sample using Procedures COP-0001, Sampling via Various
*
            Balance-Of-Plant Systems, Attachment 8, Reactor Sample Panel Routine
STP-508-4543, Turbine First Stage Pressure Channel Functional Test,
            Sample Points, Revision 14, and COP-0305, Operation of the Countroom
Revision 7, performed on June 4, 2006
            Analysis Systems, Revision 2, performed on June 15, 2006
*
  Documents reviewed by the inspectors are listed in the attachment.
Reactor coolant sample using Procedures COP-0001, Sampling via Various
  The inspectors completed six inspection samples.
Balance-Of-Plant Systems, Attachment 8, Reactor Sample Panel Routine
h. Findings
Sample Points, Revision 14, and COP-0305, Operation of the Countroom
  Introduction: The inspectors identified an NCV of TS 5.4.1.a for the failure of the
Analysis Systems, Revision 2, performed on June 15, 2006
  licensee to provide an adequate surveillance test procedure to perform TS Surveillance
Documents reviewed by the inspectors are listed in the attachment.
  Requirement (SR) 3.8.1.1. Specifically, STP-000-0102, Power Distribution Alignment
The inspectors completed six inspection samples.
  Check, Revision 4, did not include steps to verify the required offsite power circuit
    h.
  breaker alignment and indicated power availability for the Division III 4.16 kV ESF bus
Findings
  as required in Modes 1, 2, and 3.
Introduction: The inspectors identified an NCV of TS 5.4.1.a for the failure of the
  Description: As discussed in Section 1R15 of this report, operators failed to properly
licensee to provide an adequate surveillance test procedure to perform TS Surveillance
  rack in Breaker NNS-ACB23 on April 29, 2006. This condition was discovered on
Requirement (SR) 3.8.1.1. Specifically, STP-000-0102, Power Distribution Alignment
  May 22, when the breaker failed to close. During this period, on May 14, 2006, the
Check, Revision 4, did not include steps to verify the required offsite power circuit
  Division I EDG was removed from service to replace a leaking section of jacket cooling
breaker alignment and indicated power availability for the Division III 4.16 kV ESF bus  
  water vent tubing. With the Division I EDG removed from service, TS Required
as required in Modes 1, 2, and 3.  
  Action 3.8.1.a.1 required that operators perform TS SR 3.8.1.1 within one hour and
Description: As discussed in Section 1R15 of this report, operators failed to properly
  once every 8 hours until the EDG was operable. TS SR 3.8.1.1 required operators to
rack in Breaker NNS-ACB23 on April 29, 2006. This condition was discovered on
  verify the correct breaker alignment and indicated power for each required offsite power
May 22, when the breaker failed to close. During this period, on May 14, 2006, the
  circuit. Operators utilized Procedure STP-000-0102, Power Distribution Alignment
Division I EDG was removed from service to replace a leaking section of jacket cooling
  Check, Revision 4, to satisfy the requirements of TS SR 3.8.1.1; however, the
water vent tubing. With the Division I EDG removed from service, TS Required
  inspectors identified that the procedure did not have steps to verify the correct breaker
Action 3.8.1.a.1 required that operators perform TS SR 3.8.1.1 within one hour and
  alignment and indicated power availability to the Division III 4.16 kV ESF bus. As a
once every 8 hours until the EDG was operable. TS SR 3.8.1.1 required operators to
  result, the operators did not identify that Breaker NNS-ACB23 was not racked in.
verify the correct breaker alignment and indicated power for each required offsite power
  During the period that the Division I EDG was removed from service, the plant was
circuit. Operators utilized Procedure STP-000-0102, Power Distribution Alignment
  actually in TS Condition 3.8.1.d. TS Condition 3.8.1.d states that with One required
Check, Revision 4, to satisfy the requirements of TS SR 3.8.1.1; however, the
  offsite circuit inoperable AND one required [E]DG inoperable, restore the EDG or the
inspectors identified that the procedure did not have steps to verify the correct breaker
  offsite power supply to an operable status in 12 hours or place the plant in Mode 3 within
alignment and indicated power availability to the Division III 4.16 kV ESF bus. As a
  the next 12 hours. The Division I EDG was inoperable for 15 hours and 15 minutes.
result, the operators did not identify that Breaker NNS-ACB23 was not racked in.
  Procedure STP-000-0102, Section 1.1, states, in part, that its purpose is to verify the
During the period that the Division I EDG was removed from service, the plant was
  correct breaker alignment and indicated power availability for each required offsite
actually in TS Condition 3.8.1.d. TS Condition 3.8.1.d states that with One required
  power circuit in accordance with TS SR 3.8.1.1 in Modes 1, 2, and 3. TS 3.8.1 bases
offsite circuit inoperable AND one required [E]DG inoperable, restore the EDG or the
  defines an offsite power circuit as follows: Each offsite circuit consists of incoming
offsite power supply to an operable status in 12 hours or place the plant in Mode 3 within
  breakers and disconnects to the respective preferred station service Transformers 1C
the next 12 hours. The Division I EDG was inoperable for 15 hours and 15 minutes.
  and 1D [RSS1 and RSS2], the 1C and 1D preferred station service transformers, and
Procedure STP-000-0102, Section 1.1, states, in part, that its purpose is to verify the
  the respective circuit path including feeder breakers to the three 4.16 kV ESF buses.
correct breaker alignment and indicated power availability for each required offsite
                                            -21-                                      Enclosure
power circuit in accordance with TS SR 3.8.1.1 in Modes 1, 2, and 3. TS 3.8.1 bases
defines an offsite power circuit as follows: Each offsite circuit consists of incoming
breakers and disconnects to the respective preferred station service Transformers 1C
and 1D [RSS1 and RSS2], the 1C and 1D preferred station service transformers, and
the respective circuit path including feeder breakers to the three 4.16 kV ESF buses.  


Enclosure
-22-
NNS-ACB23 is one of the circuit breakers between preferred station service
NNS-ACB23 is one of the circuit breakers between preferred station service
Transformer RTX-XSR1C and the Division III 4.16 kV ESF bus.
Transformer RTX-XSR1C and the Division III 4.16 kV ESF bus.
Analysis: The performance deficiency associated with this finding involved the
Analysis: The performance deficiency associated with this finding involved the
licensees failure to provide operators with an adequate STP to meet the requirements
licensees failure to provide operators with an adequate STP to meet the requirements
of TS SR 3.8.1.1 to verify correct breaker alignment and indicated power availability to
of TS SR 3.8.1.1 to verify correct breaker alignment and indicated power availability to
the Division III ESF bus for each required offsite circuit. A review of previous revisions
the Division III ESF bus for each required offsite circuit. A review of previous revisions
of STP-000-0102 showed that the procedure has never verified the required offsite
of STP-000-0102 showed that the procedure has never verified the required offsite
power circuits for the Division III 4.16 kV ESF bus in Modes 1, 2, and 3. Although this
power circuits for the Division III 4.16 kV ESF bus in Modes 1, 2, and 3. Although this
performance deficiency caused the failure to verify the offsite power circuit for an
performance deficiency caused the failure to verify the offsite power circuit for an
extended period of time, the risk impact was limited to the 10 days from May 12-22,
extended period of time, the risk impact was limited to the 10 days from May 12-22,
2006. Therefore, the risk characterization of this finding is the same as that described in
2006. Therefore, the risk characterization of this finding is the same as that described in
Section 1R15 of this inspection report. The cause of the finding was related to the
Section 1R15 of this inspection report. The cause of the finding was related to the
crosscutting aspect of human performance because the licensee did not provide the
crosscutting aspect of human performance because the licensee did not provide the
operators with an adequate STP to complete the TS SR to verify the required offsite
operators with an adequate STP to complete the TS SR to verify the required offsite
power circuits breaker alignment to all three 4.16 kV ESF buses. Additionally, the
power circuits breaker alignment to all three 4.16 kV ESF buses. Additionally, the
cause of the finding was related to the crosscutting aspect of problem identification and
cause of the finding was related to the crosscutting aspect of problem identification and
resolution in that on two occasions, June 18, 2005, and May 22, 2006, operators
resolution in that on two occasions, June 18, 2005, and May 22, 2006, operators
Line 975: Line 1,210:
SR 3.8.1.1, but did not recognize that STP-000-0102 did not verify the other offsite
SR 3.8.1.1, but did not recognize that STP-000-0102 did not verify the other offsite
power circuit breaker alignment to the Division III 4.16 kV ESF bus.
power circuit breaker alignment to the Division III 4.16 kV ESF bus.
Enforcement: TS 5.4.1.a requires that written procedures be established, implemented,
Enforcement: TS 5.4.1.a requires that written procedures be established, implemented,
and maintained covering the activities specified in Appendix A, "Typical Procedures for
and maintained covering the activities specified in Appendix A, "Typical Procedures for
Pressurized Water Reactors and Boiling Water Reactors," of Regulatory Guide 1.33,
Pressurized Water Reactors and Boiling Water Reactors," of Regulatory Guide 1.33,
"Quality Assurance Program Requirements (Operation)," dated February 1978.
"Quality Assurance Program Requirements (Operation)," dated February 1978.  
Regulatory Guide 1.33, Appendix A, Section 8.a, requires procedures for all TS SRs.
Regulatory Guide 1.33, Appendix A, Section 8.a, requires procedures for all TS SRs.  
Procedure STP-000-0102 states that it verified the correct breaker alignment and power
Procedure STP-000-0102 states that it verified the correct breaker alignment and power
availability for each required offsite circuit in accordance with TS SR 3.8.1.1 in Modes 1,
availability for each required offsite circuit in accordance with TS SR 3.8.1.1 in Modes 1,
2, and 3. Contrary to this, Procedure STP-000-0102, Revision 4, did not require
2, and 3. Contrary to this, Procedure STP-000-0102, Revision 4, did not require
verification of the correct breaker alignment for the offsite power circuits to the
verification of the correct breaker alignment for the offsite power circuits to the
Division III 4.16 kV ESF bus in Modes 1, 2, and 3. The root cause involved the incorrect
Division III 4.16 kV ESF bus in Modes 1, 2, and 3. The root cause involved the incorrect
interpretation of the Division III 4.16 kV bus SRs as they apply to the unique River Bend
interpretation of the Division III 4.16 kV bus SRs as they apply to the unique River Bend
Station ESF electrical distribution system. The corrective actions to restore compliance
Station ESF electrical distribution system. The corrective actions to restore compliance
included as an interim measure entering in the control room logs the breaker alignment
included as an interim measure entering in the control room logs the breaker alignment
for and the bus voltage available to the Division III 4.16 kV ESF bus, until STP-000-0102
for and the bus voltage available to the Division III 4.16 kV ESF bus, until STP-000-0102
could be revised. Because the finding was of very low safety significance and has been
could be revised. Because the finding was of very low safety significance and has been
entered into the licensees CAP as CR-RBS-2006-02675 and -02402, this violation is
entered into the licensees CAP as CR-RBS-2006-02675 and -02402, this violation is
being treated as an NCV consistent with Section VI.A of the Enforcement Policy: NCV
being treated as an NCV consistent with Section VI.A of the Enforcement Policy: NCV
05000458/2006003-03, Inadequate procedure to verify required offsite power breaker
05000458/2006003-03, Inadequate procedure to verify required offsite power breaker
alignment.
alignment.
                                          -22-                                    Enclosure


1R23 Temporary Plant Modifications
Enclosure
  a. Inspection Scope
-23-
      The inspectors reviewed the USAR, plant drawings, procedure requirements, and TS to
1R23
      ensure that Temporary Alteration 2006-0011, Off Gas Pretreatment Radiation Monitor
Temporary Plant Modifications
      Sample Chamber Drain Line Modification, was properly implemented. The inspectors:
    a.
      (1) verified that the modification did not have an affect on system operability/availability;
Inspection Scope
      (2) verified that the installation was consistent with modification documents; (3) ensured
The inspectors reviewed the USAR, plant drawings, procedure requirements, and TS to
      that the postinstallation test results were satisfactory and that the impact of the
ensure that Temporary Alteration 2006-0011, Off Gas Pretreatment Radiation Monitor
      temporary modification on the operation of the pretreatment radiation monitor were
Sample Chamber Drain Line Modification, was properly implemented. The inspectors:  
      supported by the test; (4) verified that the modification was identified on control room
(1) verified that the modification did not have an affect on system operability/availability;
      drawings and that appropriate identification tags were placed on the affected drawings;
(2) verified that the installation was consistent with modification documents; (3) ensured
      and (5) verified that appropriate safety evaluations were completed. The inspectors
that the postinstallation test results were satisfactory and that the impact of the
      verified that the licensee identified and implemented any needed corrective actions
temporary modification on the operation of the pretreatment radiation monitor were
      associated with temporary modifications.
supported by the test; (4) verified that the modification was identified on control room
      The inspectors completed one inspection sample.
drawings and that appropriate identification tags were placed on the affected drawings;
  b. Findings
and (5) verified that appropriate safety evaluations were completed. The inspectors
      No findings of significance were identified.
verified that the licensee identified and implemented any needed corrective actions
      Cornerstone: Emergency Preparedness
associated with temporary modifications.
The inspectors completed one inspection sample.
    b.
Findings
No findings of significance were identified.
Cornerstone: Emergency Preparedness
1EP6 Drill Evaluation
1EP6 Drill Evaluation
  a. Inspection Scope
    a.
      On June 20, 2006, the inspectors observed the full scope exercise dress rehearsal,
Inspection Scope
      which was used to contribute to Drill/Exercise Performance and Emergency Response
On June 20, 2006, the inspectors observed the full scope exercise dress rehearsal,
      Organization Drill Performance PI. The inspectors: (1) observed the training evolution
which was used to contribute to Drill/Exercise Performance and Emergency Response
      to identify any weaknesses and deficiencies in classification, notification, and protective
Organization Drill Performance PI. The inspectors: (1) observed the training evolution
      action requirements development activities; (2) compared the identified weaknesses and
to identify any weaknesses and deficiencies in classification, notification, and protective
      deficiencies against licensee identified findings to determine whether the licensee was
action requirements development activities; (2) compared the identified weaknesses and
      properly identifying failures; and (3) determined whether licensee performance was in
deficiencies against licensee identified findings to determine whether the licensee was
      accordance with the guidance of the NEI 99-02, "Voluntary Submission of Performance
properly identifying failures; and (3) determined whether licensee performance was in
      Indicator Data," Revision 2, acceptance criteria. The scenario used was RDRL-EP-
accordance with the guidance of the NEI 99-02, "Voluntary Submission of Performance
      0602, Tornado/Loss of Offsite Power/Main Steam Line Break, dated June 16, 2006.
Indicator Data," Revision 2, acceptance criteria. The scenario used was RDRL-EP-
      Emergency [plan] implementing procedures reviewed by the inspectors included:
0602, Tornado/Loss of Offsite Power/Main Steam Line Break, dated June 16, 2006.
      *       EIP-2-001, Classification of Emergencies, Revision 13
Emergency [plan] implementing procedures reviewed by the inspectors included:
      *       EIP-2-006, Notifications, Revision 32
*
      *       EIP-2-007, Protective Action Guidelines Recommendations, Revision 21
EIP-2-001, Classification of Emergencies, Revision 13
      The inspectors completed one inspection sample.
*
                                              -23-                                    Enclosure
EIP-2-006, Notifications, Revision 32
*
EIP-2-007, Protective Action Guidelines Recommendations, Revision 21
The inspectors completed one inspection sample.


  b. Findings
Enclosure
      No findings of significance were identified.
-24-
2.   RADIATION SAFETY
    b.
      Cornerstone: Occupational Radiation Safety
Findings
No findings of significance were identified.
2.
RADIATION SAFETY
Cornerstone: Occupational Radiation Safety
2OS1 Access Control to Radiologically Significant Areas
2OS1 Access Control to Radiologically Significant Areas
  a. Inspection Scope
    a.
      This area was inspected to assess the licensees performance in implementing physical
Inspection Scope
      and administrative controls for airborne radioactivity areas, radiation areas, high
This area was inspected to assess the licensees performance in implementing physical
      radiation areas, and worker adherence to these controls. The inspector used the
and administrative controls for airborne radioactivity areas, radiation areas, high
      requirements in 10 CFR Part 20, TS, and the licensees procedures required by TS as
radiation areas, and worker adherence to these controls. The inspector used the
      criteria for determining compliance. During the inspection, the inspector interviewed the
requirements in 10 CFR Part 20, TS, and the licensees procedures required by TS as
      radiation protection manager, radiation protection supervisors, and radiation workers.
criteria for determining compliance. During the inspection, the inspector interviewed the
      The inspector performed independent radiation dose rate measurements and reviewed
radiation protection manager, radiation protection supervisors, and radiation workers.  
      the following items:
The inspector performed independent radiation dose rate measurements and reviewed
      *       PI events and associated documentation packages reported by the licensee in
the following items:
              the occupational radiation safety cornerstone
*
      *       Controls (surveys, posting, and barricades) of three radiation, high radiation, or
PI events and associated documentation packages reported by the licensee in
              airborne radioactivity areas
the occupational radiation safety cornerstone
      *       Radiation work permits, procedures, engineering controls, and air sampler
*
              locations
Controls (surveys, posting, and barricades) of three radiation, high radiation, or
      *       Conformation of electronic personal dosimeter alarm setpoints with survey
airborne radioactivity areas
              indications and plant policy; workers knowledge of required actions when their
*
              electronic personnel dosimeter noticeably malfunctions or alarms
Radiation work permits, procedures, engineering controls, and air sampler
      *       Barrier integrity and performance of engineering controls in airborne radioactivity
locations  
              areas
*
      *       Adequacy of the licensees internal dose assessment for any actual internal
Conformation of electronic personal dosimeter alarm setpoints with survey
              exposure greater than 50 millirem committed effective dose equivalent
indications and plant policy; workers knowledge of required actions when their
      *       Physical and programmatic controls for highly activated or contaminated
electronic personnel dosimeter noticeably malfunctions or alarms
              materials (nonfuel) stored within spent fuel and other storage pools.
*
      *       Self-assessments, audits, licensee event reports (LER), and special reports
Barrier integrity and performance of engineering controls in airborne radioactivity
              related to the access control program since the last inspection
areas
      *       Corrective action documents related to access controls
*
                                              -24-                                    Enclosure
Adequacy of the licensees internal dose assessment for any actual internal
exposure greater than 50 millirem committed effective dose equivalent
*
Physical and programmatic controls for highly activated or contaminated
materials (nonfuel) stored within spent fuel and other storage pools.
*
Self-assessments, audits, licensee event reports (LER), and special reports
related to the access control program since the last inspection  
*
Corrective action documents related to access controls  


    *       Licensee actions in cases of repetitive deficiencies or significant individual
Enclosure
            deficiencies
-25-
    *       Radiation work permit briefings and worker instructions
*
    *       Adequacy of radiological controls, such as required surveys, radiation protection
Licensee actions in cases of repetitive deficiencies or significant individual
            job coverage, and contamination controls during job performance
deficiencies
    *       Dosimetry placement in high radiation work areas with significant dose rate
*
            gradients
Radiation work permit briefings and worker instructions  
    *       Changes in licensee procedural controls of high dose rate - high radiation areas
*
            and very high radiation areas
Adequacy of radiological controls, such as required surveys, radiation protection
    *       Controls for special areas that have the potential to become very high radiation
job coverage, and contamination controls during job performance
            areas during certain plant operations
*
    *       Posting and locking of entrances to all accessible high dose rate - high radiation
Dosimetry placement in high radiation work areas with significant dose rate
            areas and very high radiation areas
gradients  
    *       Radiation worker and radiation protection technician performance with respect to
*
            radiation protection work requirements
Changes in licensee procedural controls of high dose rate - high radiation areas
    The inspector completed 21 of the required 21 samples.
and very high radiation areas
b. Findings
*
1. Unguarded High Radiation Area Boundary
Controls for special areas that have the potential to become very high radiation
    Introduction: The inspector reviewed a self-revealing NCV of TS 5.7.1, resulting from
areas during certain plant operations
    the licensees failure to control access to a high radiation area. The finding had very low
*
    safety significance.
Posting and locking of entrances to all accessible high dose rate - high radiation
    Description: On April 6, 2006, the licensee transferred reverse osmosis system filters
areas and very high radiation areas  
    from one elevation of the radwaste building to another. Because dose rates on the filter
*
    barrels were as high as 600 millirem per hour, the licensee assigned personnel to guard
Radiation worker and radiation protection technician performance with respect to
    the elevator entrances to prevent workers from entering high radiation areas. On this
radiation protection work requirements  
    occasion, the guards were not using radios, as was a common practice. Because of the
The inspector completed 21 of the required 21 samples.
    lack of good communication, a guard prematurely left his post in front of the 123-foot
    b.
    elevation elevator door. Coincidently, two workers attempted to board the elevator on
Findings
    the 123-foot elevation after the guard had left. The elevator carrying the barrels of
    1.
    radioactive filters stopped at the 123-foot elevation, the doors opened, and the
Unguarded High Radiation Area Boundary
    electronic dosimeters of the workers alarmed because of the high dose rates. The
Introduction: The inspector reviewed a self-revealing NCV of TS 5.7.1, resulting from
    guard returned and evacuated the workers before they accrued additional radiation
the licensees failure to control access to a high radiation area. The finding had very low
    dose. The highest dose rate recorded by an electronic alarming dosimeter was 164
safety significance.
    millirem per hour. Planned corrective action was still being evaluated by the licensee at
Description: On April 6, 2006, the licensee transferred reverse osmosis system filters
    the conclusion of the inspection.
from one elevation of the radwaste building to another. Because dose rates on the filter
                                            -25-                                      Enclosure
barrels were as high as 600 millirem per hour, the licensee assigned personnel to guard
the elevator entrances to prevent workers from entering high radiation areas. On this
occasion, the guards were not using radios, as was a common practice. Because of the
lack of good communication, a guard prematurely left his post in front of the 123-foot
elevation elevator door. Coincidently, two workers attempted to board the elevator on
the 123-foot elevation after the guard had left. The elevator carrying the barrels of
radioactive filters stopped at the 123-foot elevation, the doors opened, and the
electronic dosimeters of the workers alarmed because of the high dose rates. The
guard returned and evacuated the workers before they accrued additional radiation
dose. The highest dose rate recorded by an electronic alarming dosimeter was 164
millirem per hour. Planned corrective action was still being evaluated by the licensee at
the conclusion of the inspection.


  Analysis: The failure to control access to a high radiation area was a performance
Enclosure
  deficiency. The significance of the finding was greater than minor because it was
-26-
  associated with the occupational radiation safety attribute of exposure control and
Analysis: The failure to control access to a high radiation area was a performance
  affected the cornerstone objective, in that not controlling access to a high radiation area
deficiency. The significance of the finding was greater than minor because it was
  could increase personal exposure. Using the Occupational Radiation Safety
associated with the occupational radiation safety attribute of exposure control and
  Significance Determination Process, the inspector determined that the finding was of
affected the cornerstone objective, in that not controlling access to a high radiation area
  very low safety significance because it did not involve: (1) an as low as is reasonably
could increase personal exposure. Using the Occupational Radiation Safety
  achievable (ALARA) finding, (2) an overexposure, (3) a substantial potential for
Significance Determination Process, the inspector determined that the finding was of
  overexposure, or (4) an impaired ability to assess dose. Additionally, this finding had
very low safety significance because it did not involve: (1) an as low as is reasonably
  crosscutting aspects associated with human performance in that the failure of the
achievable (ALARA) finding, (2) an overexposure, (3) a substantial potential for
  individual to guard the elevator door directly contributed to the violation.
overexposure, or (4) an impaired ability to assess dose. Additionally, this finding had
  Enforcement: TS 5.7.1 requires each high radiation area, as defined in 10 CFR Part 20,
crosscutting aspects associated with human performance in that the failure of the
  in which the intensity of radiation is greater than 100 millirems per hour but less than
individual to guard the elevator door directly contributed to the violation.
  1000 millirems per hour, be barricaded and conspicuously posted as a high radiation
Enforcement: TS 5.7.1 requires each high radiation area, as defined in 10 CFR Part 20,
  area and entrance thereto shall be controlled by requiring issuance of a radiation work
in which the intensity of radiation is greater than 100 millirems per hour but less than
  permit. The licensee violated TS 5.7.1 when it failed to barricade and conspicuously
1000 millirems per hour, be barricaded and conspicuously posted as a high radiation
  post the elevator housing the radioactive filter barrels or maintain a guard to ensure
area and entrance thereto shall be controlled by requiring issuance of a radiation work
  workers did not enter a high radiation area. Because this failure to control a high
permit. The licensee violated TS 5.7.1 when it failed to barricade and conspicuously
  radiation area was of very low safety significance and has been entered into the
post the elevator housing the radioactive filter barrels or maintain a guard to ensure
  licensees CAP as CR-RBS-2006-01294, this violation is being treated as an NCV,
workers did not enter a high radiation area. Because this failure to control a high
  consistent with Section VI.A of the NRC Enforcement Policy:
radiation area was of very low safety significance and has been entered into the
  NCV 05000458/2006003-04, Failure to control access to a high radiation area.
licensees CAP as CR-RBS-2006-01294, this violation is being treated as an NCV,
2. Unanalyzed Airborne Radioactivity Survey
consistent with Section VI.A of the NRC Enforcement Policy:  
  Introduction: The inspector identified an NCV of 10 CFR 20.1501(a) because the
NCV 05000458/2006003-04, Failure to control access to a high radiation area.
  licensee failed to survey airborne radioactivity. The finding had very low significance.
    2.
  Description: On May 2, 2006, during the removal of local power range monitors, the
Unanalyzed Airborne Radioactivity Survey
  licensee started collecting an air sample of the work area. The air sample spanned two
Introduction: The inspector identified an NCV of 10 CFR 20.1501(a) because the
  shifts. A health physics technician on the second shift discarded the sample because
licensee failed to survey airborne radioactivity. The finding had very low significance.
  the first shift had not documented a start time. Therefore, the sample was never
Description: On May 2, 2006, during the removal of local power range monitors, the
  analyzed. However, all workers successfully passed through the portal monitors at the
licensee started collecting an air sample of the work area. The air sample spanned two
  exit of the controlled access area without alarm, confirming that no worker experienced
shifts. A health physics technician on the second shift discarded the sample because
  an uptake of radioactive material. Planned corrective action is still being evaluated.
the first shift had not documented a start time. Therefore, the sample was never
  Analysis: The failure to survey airborne radioactivity was a performance deficiency.
analyzed. However, all workers successfully passed through the portal monitors at the
  This finding was greater than minor because it was associated with the occupational
exit of the controlled access area without alarm, confirming that no worker experienced
  radiation safety program attribute of exposure control and affected the cornerstone
an uptake of radioactive material. Planned corrective action is still being evaluated.
  objective in that the lack of knowledge of radiological conditions could increase
Analysis: The failure to survey airborne radioactivity was a performance deficiency.  
  personnel dose. Using the Occupational Radiation Safety Significance Determination
This finding was greater than minor because it was associated with the occupational
  Process, the inspector determined that the finding was of very low safety significance
radiation safety program attribute of exposure control and affected the cornerstone
  because it did not involve: (1) an ALARA finding, (2) an overexposure, (3) a substantial
objective in that the lack of knowledge of radiological conditions could increase
  potential for overexposure, or (4) an impaired ability to assess dose. Additionally, this
personnel dose. Using the Occupational Radiation Safety Significance Determination
  finding had crosscutting aspects associated with human performance in that the failure
Process, the inspector determined that the finding was of very low safety significance
  to maintain the sample for analysis directly contributed to the violation.
because it did not involve: (1) an ALARA finding, (2) an overexposure, (3) a substantial
                                            -26-                                    Enclosure
potential for overexposure, or (4) an impaired ability to assess dose.   Additionally, this
finding had crosscutting aspects associated with human performance in that the failure
to maintain the sample for analysis directly contributed to the violation.


    Enforcement: 10 CFR 20.1501(a) requires that each licensee make or cause to be
Enclosure
    made surveys that may be necessary for the licensee to comply with the regulations in
-27-
    10 CFR Part 20 and that are reasonable under the circumstances to evaluate the extent
Enforcement: 10 CFR 20.1501(a) requires that each licensee make or cause to be
    of radiation levels, concentrations or quantities of radioactive materials, and the potential
made surveys that may be necessary for the licensee to comply with the regulations in
    radiological hazards that could be present. Pursuant to 10 CFR 20.1003, a survey
10 CFR Part 20 and that are reasonable under the circumstances to evaluate the extent
    means an evaluation of the radiological conditions and potential hazards incident to the
of radiation levels, concentrations or quantities of radioactive materials, and the potential
    production, use, transfer, release, disposal, or presence of radioactive material or other
radiological hazards that could be present. Pursuant to 10 CFR 20.1003, a survey
    sources of radiation. In part, 10 CFR 20.1201(a) states that the licensee shall control
means an evaluation of the radiological conditions and potential hazards incident to the
    the occupational dose to individual adults. The licensee violated 10 CFR 20.1501(a)
production, use, transfer, release, disposal, or presence of radioactive material or other
    when it failed to perform an evaluation of airborne radioactivity to ensure compliance
sources of radiation. In part, 10 CFR 20.1201(a) states that the licensee shall control
    with 10 CFR 20.1201(a). Because this failure to perform a radiological survey was of
the occupational dose to individual adults. The licensee violated 10 CFR 20.1501(a)
    very low safety significance and has been entered into the licensees CAP as
when it failed to perform an evaluation of airborne radioactivity to ensure compliance
    CR-RBS-2006-01994, this violation is being treated as an NCV, consistent with
with 10 CFR 20.1201(a). Because this failure to perform a radiological survey was of
    Section VI.A of the NRC Enforcement Policy: NCV 05000458/2006003-05, Failure to
very low safety significance and has been entered into the licensees CAP as
    perform airborne radiation survey.
CR-RBS-2006-01994, this violation is being treated as an NCV, consistent with
Section VI.A of the NRC Enforcement Policy: NCV 05000458/2006003-05, Failure to
perform airborne radiation survey.
2OS2 ALARA Planning and Controls
2OS2 ALARA Planning and Controls
  a. Inspection Scope
    a.
    The inspector assessed licensee performance with respect to maintaining individual and
Inspection Scope
    collective radiation exposures ALARA. The inspector used the requirements in 10 CFR
The inspector assessed licensee performance with respect to maintaining individual and
    Part 20 and the licensees procedures required by TS as criteria for determining
collective radiation exposures ALARA. The inspector used the requirements in 10 CFR
    compliance. The inspector interviewed licensee personnel and reviewed:
Part 20 and the licensees procedures required by TS as criteria for determining
    *       Current 3-year rolling average collective exposure
compliance. The inspector interviewed licensee personnel and reviewed:
    *       Three outage or on-line maintenance work activities scheduled during the
*
            inspection period and associated work activity exposure estimates which were
Current 3-year rolling average collective exposure  
            likely to result in the highest personnel collective exposures
*
    *       ALARA work activity evaluations, exposure estimates, and exposure mitigation
Three outage or on-line maintenance work activities scheduled during the
            requirements
inspection period and associated work activity exposure estimates which were
    *       Intended versus actual work activity doses and the reasons for any
likely to result in the highest personnel collective exposures  
            inconsistencies
*
    *       Shielding requests and dose/benefit analyses
ALARA work activity evaluations, exposure estimates, and exposure mitigation
    *       Dose rate reduction activities in work planning
requirements
    *       Use of engineering controls to achieve dose reductions and dose reduction
*
            benefits afforded by shielding
Intended versus actual work activity doses and the reasons for any
    *       Workers use of the low dose waiting areas
inconsistencies  
    *       First-line job supervisors contribution to ensuring work activities are conducted
*
            in a dose efficient manner
Shielding requests and dose/benefit analyses
                                              -27-                                    Enclosure
*
Dose rate reduction activities in work planning  
*
Use of engineering controls to achieve dose reductions and dose reduction
benefits afforded by shielding  
*
Workers use of the low dose waiting areas
*
First-line job supervisors contribution to ensuring work activities are conducted
in a dose efficient manner  


      *       Radiation worker and radiation protection technician performance during work
Enclosure
              activities in radiation areas, airborne radioactivity areas, or high radiation areas
-28-
      The inspector completed 6 of the required 15 samples and 4 of the optional samples.
*
    b. Findings
Radiation worker and radiation protection technician performance during work
      No findings of significance were identified.
activities in radiation areas, airborne radioactivity areas, or high radiation areas  
4.     OTHER ACTIVITIES
The inspector completed 6 of the required 15 samples and 4 of the optional samples.  
    b.
Findings
No findings of significance were identified.
4.
OTHER ACTIVITIES
4OA1 Performance Indicator Verification
4OA1 Performance Indicator Verification
    a. Inspection Scope
    a.
  1. Barrier Integrity Cornerstone
Inspection Scope
      The inspectors sampled licensee submittals for the two PIs listed below for the period
    1.
      October 1, 2004, through March 31, 2006. The definitions and guidance of NEI 99-02,
Barrier Integrity Cornerstone
      Regulatory Assessment Indicator Guideline, Revision 4, were used to verify the
The inspectors sampled licensee submittals for the two PIs listed below for the period
      licensees basis for reporting each data element in order to verify the accuracy of PI
October 1, 2004, through March 31, 2006. The definitions and guidance of NEI 99-02,
      data reported during the assessment period. The inspectors: (1) reviewed reactor
Regulatory Assessment Indicator Guideline, Revision 4, were used to verify the
      coolant system (RCS) chemistry sample analyses for dose equivalent Iodine-131 and
licensees basis for reporting each data element in order to verify the accuracy of PI
      compared the results to the TS limit; (2) observed a chemistry technician obtain and
data reported during the assessment period. The inspectors: (1) reviewed reactor
      analyze an RCS sample; (3) reviewed operating logs and surveillance results for
coolant system (RCS) chemistry sample analyses for dose equivalent Iodine-131 and
      measurements of RCS identified leakage; and (4) observed a surveillance test that
compared the results to the TS limit; (2) observed a chemistry technician obtain and
      determined RCS identified leakage.
analyze an RCS sample; (3) reviewed operating logs and surveillance results for
      C       RCS Specific Activity
measurements of RCS identified leakage; and (4) observed a surveillance test that
      C       RCS Leakage
determined RCS identified leakage.
      The inspectors completed two inspection samples.
C
  2. Occupational Radiation Safety Cornerstone
RCS Specific Activity
      The review included corrective action documentation that identified occurrences in
C
      locked high radiation areas (as defined in the licensees TS), very high radiation areas
RCS Leakage
      (as defined in 10 CFR 20.1003), and unplanned personnel exposures (as defined in
The inspectors completed two inspection samples.
      NEI 99-02), specifically CR-RBS-2006-01910. Additional records reviewed included
    2.
      ALARA records and whole-body counts of selected individual exposures. The inspector
Occupational Radiation Safety Cornerstone
      interviewed licensee personnel that were accountable for collecting and evaluating the
The review included corrective action documentation that identified occurrences in
      PI data. In addition, the inspector toured plant areas to verify that high radiation, locked
locked high radiation areas (as defined in the licensees TS), very high radiation areas
      high radiation, and very high radiation areas were properly controlled. PI definitions and
(as defined in 10 CFR 20.1003), and unplanned personnel exposures (as defined in
      guidance contained in NEI 99-02, "Regulatory Assessment Indicator Guideline,"
NEI 99-02), specifically CR-RBS-2006-01910. Additional records reviewed included
      Revision 3, were used to verify the basis in reporting for each data element.
ALARA records and whole-body counts of selected individual exposures. The inspector
                                                -28-                                      Enclosure
interviewed licensee personnel that were accountable for collecting and evaluating the
PI data. In addition, the inspector toured plant areas to verify that high radiation, locked
high radiation, and very high radiation areas were properly controlled. PI definitions and
guidance contained in NEI 99-02, "Regulatory Assessment Indicator Guideline,"
Revision 3, were used to verify the basis in reporting for each data element.


      *       Occupational Exposure Control Effectiveness
Enclosure
      The inspector completed the one required sample in this cornerstone.
-29-
  3. Public Radiation Safety Cornerstone
*
      The inspector reviewed licensee documents from June 1, 2005, through March 31,
Occupational Exposure Control Effectiveness
      2006. Licensee records reviewed included corrective action documentation that
The inspector completed the one required sample in this cornerstone.
      identified occurrences for liquid or gaseous effluent releases that exceeded PI
    3.
      thresholds and those reported to the NRC. The inspector interviewed licensee
Public Radiation Safety Cornerstone
      personnel that were accountable for collecting and evaluating the PI data. PI definitions
The inspector reviewed licensee documents from June 1, 2005, through March 31,
      and guidance contained in NEI 99-02, "Regulatory Assessment Indicator Guideline,"
2006. Licensee records reviewed included corrective action documentation that
      Revision 3, were used to verify the basis in reporting for each data element.
identified occurrences for liquid or gaseous effluent releases that exceeded PI
      *       Radiological Effluent Technical Specification/Offsite Dose Calculation Manual
thresholds and those reported to the NRC. The inspector interviewed licensee
              Radiological Effluent Occurrences
personnel that were accountable for collecting and evaluating the PI data. PI definitions
      The inspector completed the one required sample in this cornerstone.
and guidance contained in NEI 99-02, "Regulatory Assessment Indicator Guideline,"
  f. Findings
Revision 3, were used to verify the basis in reporting for each data element.
      No findings of significance were identified.
*
Radiological Effluent Technical Specification/Offsite Dose Calculation Manual  
Radiological Effluent Occurrences  
The inspector completed the one required sample in this cornerstone.
    f.
Findings
No findings of significance were identified.
4OA2 Identification and Resolution of Problems
4OA2 Identification and Resolution of Problems
1.   Semiannual Trend Review
  1.
  g. Inspection Scope
Semiannual Trend Review
      The inspectors completed a semiannual trend review of repetitive or closely related
    g.
      issues related to identify trends that might indicate the existence of more safety
Inspection Scope
      significant issues. The inspectors review consisted of the 6-month period from
The inspectors completed a semiannual trend review of repetitive or closely related
      January 1 to June 30, 2006, of CAP items associated with the three EDG starting air
issues related to identify trends that might indicate the existence of more safety
      systems documented in 42 CRs. When warranted, some of the samples expanded
significant issues. The inspectors review consisted of the 6-month period from
      beyond those dates to fully assess the issue. The inspectors compared and contrasted
January 1 to June 30, 2006, of CAP items associated with the three EDG starting air
      their results with the results contained in adverse trend CRs for problems related to the
systems documented in 42 CRs. When warranted, some of the samples expanded
      starting air compressors and air dryers. Corrective actions associated with a sample of
beyond those dates to fully assess the issue. The inspectors compared and contrasted
      the issues identified were reviewed for adequacy. The CRs reviewed by the inspectors
their results with the results contained in adverse trend CRs for problems related to the
      are listed in the attachment.
starting air compressors and air dryers. Corrective actions associated with a sample of
      The inspectors completed one inspection sample.
the issues identified were reviewed for adequacy. The CRs reviewed by the inspectors
  b. Findings and Observations
are listed in the attachment.
      There were no findings of significance identified associated with the CRs reviewed.
The inspectors completed one inspection sample.
      The inspectors noted that the licensee had identified a long-standing issue related to the
    b. Findings and Observations
      performance of the EDG starting air systems air compressors. Since January 1, 2006,
There were no findings of significance identified associated with the CRs reviewed.
                                              -29-                                  Enclosure
The inspectors noted that the licensee had identified a long-standing issue related to the
performance of the EDG starting air systems air compressors. Since January 1, 2006,


      there were 18 CRs written for high metal wear products in monthly air compressor oil
Enclosure
      samples. Each of these CRs was closed to CR-RBS-2004-02165. An additional
-30-
      28 CRs written since August 2, 2004, for high metal wear product concentrations and
there were 18 CRs written for high metal wear products in monthly air compressor oil
      high moisture content in monthly compressor oil samples were closed to CR-RBS-2004-
samples. Each of these CRs was closed to CR-RBS-2004-02165. An additional
      02165. In addition, operators wrote adverse trend CR-RBS-2006-02407 to detail
28 CRs written since August 2, 2004, for high metal wear product concentrations and
      compressor problems, including excessive run times. The inspectors determined that
high moisture content in monthly compressor oil samples were closed to CR-RBS-2004-
      the licensee is taking appropriate actions to understand the problem with the EDG
02165. In addition, operators wrote adverse trend CR-RBS-2006-02407 to detail
      starting air compressors, including sending the system engineer to observe the vendors
compressor problems, including excessive run times. The inspectors determined that
      teardown and refurbishment of two of the starting air compressors.
the licensee is taking appropriate actions to understand the problem with the EDG
      Another four CRs have been written since January 1, 2006, describing problems with
starting air compressors, including sending the system engineer to observe the vendors
      starting air system dryers and dryer prefilters. Following a June 29, 2006, meeting held
teardown and refurbishment of two of the starting air compressors.
      to discuss overall EDG starting air system maintenance problems, the licensee wrote
Another four CRs have been written since January 1, 2006, describing problems with
      CR-RBS-2006-02799, to look into the relationship between the prefilter and dryer
starting air system dryers and dryer prefilters. Following a June 29, 2006, meeting held
      problems. The inspectors noted that this meeting was the first discussion of the overall
to discuss overall EDG starting air system maintenance problems, the licensee wrote
      condition of the EDG starting air systems and to evaluate the interrelationship between
CR-RBS-2006-02799, to look into the relationship between the prefilter and dryer
      compressor, dryer, and prefilter problems.
problems. The inspectors noted that this meeting was the first discussion of the overall
2.   Occupational Radiation Safety
condition of the EDG starting air systems and to evaluate the interrelationship between
  a. Inspection Scope
compressor, dryer, and prefilter problems.
      The inspector evaluated the effectiveness of the licensees problem identification and
  2.
      resolution process with respect to the following inspection areas:
Occupational Radiation Safety
      *       Access Control to Radiologically Significant Areas (Section 2OS1)
    a.
      *       ALARA Planning and Controls (Section 2OS2)
Inspection Scope
  b. Findings and Observations
The inspector evaluated the effectiveness of the licensees problem identification and
      No findings of significance were identified.
resolution process with respect to the following inspection areas:
3.   Inservice Inspection Activities
*
  a. Inspection Scope
Access Control to Radiologically Significant Areas (Section 2OS1)
      The inspector reviewed selected inservice inspection related CRs issued during the
*
      current and past refueling outages. The review served to verify that the licensees CAP
ALARA Planning and Controls (Section 2OS2)
      was being correctly utilized to identify conditions adverse to quality and that those
    b. Findings and Observations
      conditions were being adequately evaluated, corrected, and trended.
No findings of significance were identified.
  b. Findings
  3.
      No findings of significance were identified.
Inservice Inspection Activities
                                              -30-                                    Enclosure
    a.
Inspection Scope
The inspector reviewed selected inservice inspection related CRs issued during the
current and past refueling outages. The review served to verify that the licensees CAP
was being correctly utilized to identify conditions adverse to quality and that those
conditions were being adequately evaluated, corrected, and trended.
    b.
Findings
No findings of significance were identified.


Enclosure
-31-
4OA3 Event Followup
4OA3 Event Followup
  1. (Closed) LER 50-458/2004-003-01, Unplanned Automatic Start of Standby Diesel
    1.
    Generator Due to Loss of Division 1 Switchgear
(Closed) LER 50-458/2004-003-01, Unplanned Automatic Start of Standby Diesel
    On October 31, 2004, technicians caused an unexpected degraded voltage signal,
Generator Due to Loss of Division 1 Switchgear
    which resulted in a loss of the Division I 4.16 kV ESF bus during preparations for the
On October 31, 2004, technicians caused an unexpected degraded voltage signal,
    Division I loss of offsite power/loss of coolant accident test. The Division I EDG
which resulted in a loss of the Division I 4.16 kV ESF bus during preparations for the
    automatically started and powered the ESF bus and all equipment operated as
Division I loss of offsite power/loss of coolant accident test. The Division I EDG
    expected. Initial inspection of this event was documented in NRC integrated inspection
automatically started and powered the ESF bus and all equipment operated as
    Report 05000458/2004005. During this inspection period, the inspectors reviewed the
expected. Initial inspection of this event was documented in NRC integrated inspection
    LER, the root cause analysis, and corrective actions documented in
Report 05000458/2004005. During this inspection period, the inspectors reviewed the
    CR-RBS-2004-03518. No additional findings of significance were identified. This LER
LER, the root cause analysis, and corrective actions documented in
    is closed.
CR-RBS-2004-03518. No additional findings of significance were identified. This LER
  2. (Closed) LER 50-458/2004-004-01, Unplanned Automatic Start of Standby Diesel
is closed.
    Generator Due to Loss of Division 2 Switchgear
    2.
    On November 1, 2004, technicians inadvertently caused a trip of Transformer RSS2
(Closed) LER 50-458/2004-004-01, Unplanned Automatic Start of Standby Diesel
    preferred station service Transformer RTX-XSR1F while troubleshooting a transformer
Generator Due to Loss of Division 2 Switchgear
    sudden pressure relay trip circuit. As a result, power was also lost to preferred station
On November 1, 2004, technicians inadvertently caused a trip of Transformer RSS2
    Transformer RTX-XSR1D and the Division II 4.16 kV ESF bus. The running shutdown
preferred station service Transformer RTX-XSR1F while troubleshooting a transformer
    cooling, alternate decay heat removal, and plant operating water cleanup systems lost
sudden pressure relay trip circuit. As a result, power was also lost to preferred station
    power until the Division II EDG started and restored power to the ESF bus. Shutdown
Transformer RTX-XSR1D and the Division II 4.16 kV ESF bus. The running shutdown
    cooling was restored in less than one hour. Initial inspection of this event was
cooling, alternate decay heat removal, and plant operating water cleanup systems lost
    documented in NRC integrated inspection Report 05000458/2004005. During this
power until the Division II EDG started and restored power to the ESF bus. Shutdown
    inspection period, the inspectors reviewed the LER, the root cause analysis, and
cooling was restored in less than one hour. Initial inspection of this event was
    corrective actions documented in CR-RBS-2004-03546. No additional findings of
documented in NRC integrated inspection Report 05000458/2004005. During this
    significance were identified. This LER is closed.
inspection period, the inspectors reviewed the LER, the root cause analysis, and
  3. (Closed) LER 50-458/2004-005-01, Unplanned Automatic Scram Due to Loss of
corrective actions documented in CR-RBS-2004-03546. No additional findings of
    Non-Vital 120 Volt Instrument Bus
significance were identified. This LER is closed.
    On December 10, 2004, an automatic scram occurred due to a loss of power to
    3.
    nonsafety-related instrumentation Bus VBN-PNL01B1. A capacitor on the control board
(Closed) LER 50-458/2004-005-01, Unplanned Automatic Scram Due to Loss of
    for the nonsafety-related Inverter BYS-INV01B static switch failed, which caused a loss
Non-Vital 120 Volt Instrument Bus
    of power to Bus VBN-PNL01B1, a subsequent downshift of the plant operating
On December 10, 2004, an automatic scram occurred due to a loss of power to
    recirculation pumps and a lockup of the main feedwater regulating valves. The result
nonsafety-related instrumentation Bus VBN-PNL01B1. A capacitor on the control board
    was an automatic plant scram complicated by a loss of normal feedwater. Inspection of
for the nonsafety-related Inverter BYS-INV01B static switch failed, which caused a loss
    this event was documented in NRC integrated inspection Report 05000458/2004005.
of power to Bus VBN-PNL01B1, a subsequent downshift of the plant operating
    Additional inspection was documented in NRC supplemental inspection Report
recirculation pumps and a lockup of the main feedwater regulating valves. The result
    05000458/2005012. During this inspection period, the inspectors reviewed the LER, the
was an automatic plant scram complicated by a loss of normal feedwater. Inspection of
    root cause analysis, and corrective actions documented in CR-RBS-2004-04289. No
this event was documented in NRC integrated inspection Report 05000458/2004005.  
    additional findings of significance were identified. This LER is closed.
Additional inspection was documented in NRC supplemental inspection Report
                                              -31-                                    Enclosure
05000458/2005012. During this inspection period, the inspectors reviewed the LER, the
root cause analysis, and corrective actions documented in CR-RBS-2004-04289. No
additional findings of significance were identified. This LER is closed.


  4. (Closed) LER 50-458 /2005-001-01, Unplanned Manual Scram Due to Indication of
Enclosure
      Ground Fault in Main Generator
-32-
      On January 15, 2005, while the plant was at 100 percent power, a main generator field
    4.
      ground fault alarm was received. Control room operators tripped the turbine in
(Closed) LER 50-458 /2005-001-01, Unplanned Manual Scram Due to Indication of
      accordance with alarm response Procedure ARP-680-09. The licensee later determined
Ground Fault in Main Generator
      that one of the five rectifier banks in the generator excitation control system was the
On January 15, 2005, while the plant was at 100 percent power, a main generator field
      source of the ground and removed it from service. In addition, the licensee tested the
ground fault alarm was received. Control room operators tripped the turbine in
      relay that causes the main generator ground fault alarm and found it to be out of
accordance with alarm response Procedure ARP-680-09. The licensee later determined
      calibration such that it alarmed before the ground current reached its setpoint. The
that one of the five rectifier banks in the generator excitation control system was the
      alarm response procedure requirement to trip the turbine was revised to allow validation
source of the ground and removed it from service. In addition, the licensee tested the
      of the alarm before tripping the main turbine. Inspection of this event was documented
relay that causes the main generator ground fault alarm and found it to be out of
      in NRC integrated inspection Report 05000458/2005002. Additional inspection was
calibration such that it alarmed before the ground current reached its setpoint. The
      documented in NRC supplemental inspection Report 05000458/2005012. During this
alarm response procedure requirement to trip the turbine was revised to allow validation
      inspection period, the inspectors reviewed the LER, the root cause analysis, and
of the alarm before tripping the main turbine. Inspection of this event was documented
      corrective actions documented in CR-RBS-2005-00140. No additional findings of
in NRC integrated inspection Report 05000458/2005002. Additional inspection was
      significance were identified. This LER is closed.
documented in NRC supplemental inspection Report 05000458/2005012. During this
inspection period, the inspectors reviewed the LER, the root cause analysis, and
corrective actions documented in CR-RBS-2005-00140. No additional findings of
significance were identified. This LER is closed.
4OA5 Other Activities
4OA5 Other Activities
      Implementation of Temporary Instruction 2515/165 - Operational Readiness of Offsite
Implementation of Temporary Instruction 2515/165 - Operational Readiness of Offsite
      Power and Impact on Plant Risk
Power and Impact on Plant Risk
  a. Inspection Scope
    a.
      The objective of Temporary Instruction 2515/165, "Operational Readiness of Offsite
Inspection Scope
      Power and Impact on Plant Risk," was to gather information to support the assessment
The objective of Temporary Instruction 2515/165, "Operational Readiness of Offsite
      of nuclear power plant operational readiness of offsite power systems and impact on
Power and Impact on Plant Risk," was to gather information to support the assessment
      plant risk. During this inspection, the inspectors interviewed licensee personnel,
of nuclear power plant operational readiness of offsite power systems and impact on
      reviewed licensee procedures, and gathered information for further evaluation by the
plant risk. During this inspection, the inspectors interviewed licensee personnel,
      Office of Nuclear Reactor Regulation.
reviewed licensee procedures, and gathered information for further evaluation by the
  b. Findings
Office of Nuclear Reactor Regulation.  
      No findings of significance were identified.
    b.
Findings
No findings of significance were identified.
4OA6 Meetings, Including Exit
4OA6 Meetings, Including Exit
      Exit Meetings
Exit Meetings
      On May 5, 2006, the inspector presented the occupational radiation safety inspection
On May 5, 2006, the inspector presented the occupational radiation safety inspection
      results to Mr. D. Vinci, General Manager, Plant Operations, and other members of his
results to Mr. D. Vinci, General Manager, Plant Operations, and other members of his
      staff who acknowledged the findings. The inspector confirmed that proprietary
staff who acknowledged the findings. The inspector confirmed that proprietary
      information was not provided or examined during the inspection.
information was not provided or examined during the inspection.
      On May 5, 2006, the inspector presented the results of this inspection of inservice
On May 5, 2006, the inspector presented the results of this inspection of inservice
      inspection activities to Mr. P. Russell, Manager, System Engineering, and other
inspection activities to Mr. P. Russell, Manager, System Engineering, and other
                                                -32-                                  Enclosure


    members of licensee management. The inspector confirmed that proprietary
Enclosure
    information was not provided or examined during the inspection.
-33-
    On July 5, 2006, the resident inspectors presented the integrated baseline inspection
members of licensee management. The inspector confirmed that proprietary
    results to Mr. P. Hinnenkamp, Vice President - Operations, and other members of
information was not provided or examined during the inspection.
    licensee management. The inspectors confirmed that proprietary information was not
On July 5, 2006, the resident inspectors presented the integrated baseline inspection
    provided or examined during the inspection.
results to Mr. P. Hinnenkamp, Vice President - Operations, and other members of
ATTACHMENT: SUPPLEMENTAL INFORMATION
licensee management. The inspectors confirmed that proprietary information was not
                                          -33-                                    Enclosure
provided or examined during the inspection.
ATTACHMENT: SUPPLEMENTAL INFORMATION


                              SUPPLEMENTAL INFORMATION
Attachment
                                  KEY POINTS OF CONTACT
A-1
SUPPLEMENTAL INFORMATION
KEY POINTS OF CONTACT
Licensee Personnel
Licensee Personnel
T. Baccus, Acting Supervisor, ALARA Planning
T. Baccus, Acting Supervisor, ALARA Planning
Line 1,405: Line 1,719:
C. Stafford, Manager, Operations
C. Stafford, Manager, Operations
D. Vinci, General Manager - Plant Operations
D. Vinci, General Manager - Plant Operations
                    LIST OF ITEMS OPENED, CLOSED, AND DISCUSSED
LIST OF ITEMS OPENED, CLOSED, AND DISCUSSED
Opened and Closed
Opened and Closed
05000458/2006003-01           NCV   Failure to identify Division III ESF bus supply breaker not
05000458/2006003-01
                                    racked in
NCV
05000458/2006003-02           NCV   Failure to adequately manage an increase in plant risk
Failure to identify Division III ESF bus supply breaker not
05000458/2006003-03           NCV   Inadequate procedure to verify required offsite power
racked in
                                    breaker alignment
05000458/2006003-02
05000458/2006003-04           NCV   Failure to control access to a high radiation area
NCV
05000458/2006003-05           NCV   Failure to perform airborne radiation survey
Failure to adequately manage an increase in plant risk  
                                              A-1                                    Attachment
05000458/2006003-03
NCV
Inadequate procedure to verify required offsite power
breaker alignment
05000458/2006003-04
NCV
Failure to control access to a high radiation area
05000458/2006003-05
NCV  
Failure to perform airborne radiation survey


Attachment
A-2
Closed
Closed
50-458/2004-003-01           LER     Unplanned Automatic Start of Standby Diesel Generator
50-458/2004-003-01
                                    Due to Loss of Division 1 Switchgear
LER
50-458/2004-004-01           LER     Unplanned Automatic Start of Standby Diesel Generator
Unplanned Automatic Start of Standby Diesel Generator
                                    Due to Loss of Division 2 Switchgear
Due to Loss of Division 1 Switchgear
50-458/2004-005-01           LER     Unplanned Automatic Scram Due to Loss of Non-Vital 120
50-458/2004-004-01
                                    Volt Instrument Bus
LER  
50-458 /2005-001-01         LER     Unplanned Manual Scram Due to Indication of Ground
Unplanned Automatic Start of Standby Diesel Generator
                                    Fault in Main Generator
Due to Loss of Division 2 Switchgear
                              LIST OF DOCUMENTS REVIEWED
50-458/2004-005-01
LER
Unplanned Automatic Scram Due to Loss of Non-Vital 120
Volt Instrument Bus
50-458 /2005-001-01
LER
Unplanned Manual Scram Due to Indication of Ground
Fault in Main Generator
LIST OF DOCUMENTS REVIEWED
The following documents were selected and reviewed by the inspectors to accomplish the
The following documents were selected and reviewed by the inspectors to accomplish the
objectives and scope of the inspection and to support any findings:
objectives and scope of the inspection and to support any findings:
Section 1R06: Inservice Inspection Activities
Section 1R06: Inservice Inspection Activities
Procedures
Procedures
CEP-NDE-0400, Ultrasonic Examination, Revision 0
CEP-NDE-0400, Ultrasonic Examination, Revision 0
Line 1,443: Line 1,776:
CEP-NDE-0731, Magnetic Particle Examination (ASME Section XI), Revision 0
CEP-NDE-0731, Magnetic Particle Examination (ASME Section XI), Revision 0
SPP-7010, Preparation of Weld Data Documents, Revision 9
SPP-7010, Preparation of Weld Data Documents, Revision 9
                                              A-2                                Attachment


Attachment
Miscellaneous Documents
Miscellaneous Documents
7228.000-701-131A, Risk Informed Break Exclusion Region Evaluation for River Bend
7228.000-701-131A, Risk Informed Break Exclusion Region Evaluation for River Bend
Station, Revision 0
Station, Revision 0
Liquid Penetrant Examinations
Liquid Penetrant Examinations
BOP-PT-06-024         BOP-PT-06-025         BOP-PT-06-026         BOP-PT-06-029
BOP-PT-06-024
BOP-PT-06-025
BOP-PT-06-026
BOP-PT-06-029
UT Calibration Reports
UT Calibration Reports
CAL -06-015                   CAL -06-016                 CAL-06-017
CAL -06-015
CAL -06-016
CAL-06-017
UT Pipe Weld Examinations
UT Pipe Weld Examinations
ISI-UT-06-003         ISI-UT-06-006         ISI-UT-06-009         ISI-UT-06-012
ISI-UT-06-003
ISI-UT-06-004         ISI-UT-06-007         ISI-UT-06-010         ISI-UT-06-013
ISI-UT-06-006
ISI-UT-06-005         ISI-UT-06-008         ISI-UT-06-011         ISI-UT-06-014
ISI-UT-06-009
ISI-UT-06-012
ISI-UT-06-004
ISI-UT-06-007
ISI-UT-06-010
ISI-UT-06-013
ISI-UT-06-005
ISI-UT-06-008
ISI-UT-06-011
ISI-UT-06-014
Condition Reports
Condition Reports
CR-RBS-2005-00065     CR-RBS-2005-00067     CR-RBS-2005-00100     CR-RBS-2005-01379
CR-RBS-2005-00065
Section 1R15: Operability Evaluations
CR-RBS-2005-00067
CR-RBS-2005-00100
CR-RBS-2005-01379
Section 1R15: Operability Evaluations
Primary Containment Purge Exhaust Line Operability
Primary Containment Purge Exhaust Line Operability
CR-RBS-2006-00964, primary containment purge exhaust line leak rate test results showing
CR-RBS-2006-00964, primary containment purge exhaust line leak rate test results showing
Line 1,470: Line 1,820:
RBS TS Amendment 81, dated July 20, 1995
RBS TS Amendment 81, dated July 20, 1995
RBS TS Bases Revision 126, dated March 31, 206
RBS TS Bases Revision 126, dated March 31, 206
                                                                                Attachment


Attachment
A-4
NNS-ACB23 Not Functional
NNS-ACB23 Not Functional
Electrical Drawings
Electrical Drawings
Line 1,478: Line 1,829:
Revision 13
Revision 13
Corrective Action Documents
Corrective Action Documents
CR-RBS-2006-02402           CR-RBS-2006-0235               CR-RBS-2006-02337
CR-RBS-2006-02402
CR-RBS-2006-0235
CR-RBS-2006-02337
CR-RBS-1998-00190
CR-RBS-1998-00190
Procedures
Procedures
Line 1,486: Line 1,839:
STP-000-0102, Power Distribution Alignment Check, Revision 4, performed on May 22, 2006
STP-000-0102, Power Distribution Alignment Check, Revision 4, performed on May 22, 2006
Work Requests
Work Requests
WR 76625             WR 77441               WR77478
WR 76625
WR 77441
WR77478
Miscellaneous Documents
Miscellaneous Documents
Main Control Room Logs
Main Control Room Logs
TS LCO Records: 1-OPT-06-0187 1-TS-06-0694
TS LCO Records: 1-OPT-06-0187
1-TS-06-0694
RBS Tagout Record: 1-302-NNS-SWG1A-006-A
RBS Tagout Record: 1-302-NNS-SWG1A-006-A
Section 1R20: Refueling and Other Outage Activities
Section 1R20: Refueling and Other Outage Activities
Procedures
Procedures
RSP-0217, Auxiliary Access Control Functions, Revision 27
RSP-0217, Auxiliary Access Control Functions, Revision 27
Line 1,500: Line 1,856:
OSP-0034, Control of Obstructions for Primary Containment/Fuel Building Operability,
OSP-0034, Control of Obstructions for Primary Containment/Fuel Building Operability,
Revision 3
Revision 3
                                              A-4                                Attachment


Attachment
A-5
GOP-0001, Plant Startup, Revision 47, performed on May 12, 2006
GOP-0001, Plant Startup, Revision 47, performed on May 12, 2006
Corrective Action Documents
Corrective Action Documents
CR-RBS-2006-00691           CR-RBS-2006-01937
CR-RBS-2006-00691
CR-RBS-2006-01937
Miscellaneous Documents
Miscellaneous Documents
Control Room Logs
Control Room Logs
Line 1,517: Line 1,875:
WO 5034041, Configure the station blackout diesel to supply power to spent fuel pool cooling
WO 5034041, Configure the station blackout diesel to supply power to spent fuel pool cooling
Pump SFC-P1A, written May 3, 2006
Pump SFC-P1A, written May 3, 2006
Section 1R22: Surveillance Testing
Section 1R22: Surveillance Testing
Drawing EE-001AC, Startup Electrical Distribution Chart, Revision 33
Drawing EE-001AC, Startup Electrical Distribution Chart, Revision 33
TS Section 3.8.1 and Bases 3.8.1, Revision 0
TS Section 3.8.1 and Bases 3.8.1, Revision 0
Line 1,524: Line 1,882:
dated May 1984
dated May 1984
TS LCO Logs
TS LCO Logs
1-TS-06-0694         I-TS-06-0685         1-TS-05-0386
1-TS-06-0694
I-TS-06-0685
1-TS-05-0386
Corrective Action Documents
Corrective Action Documents
CR-RBS-2006-02675           CR-RBS-2006-02402             CR-RBS-2005-02331
CR-RBS-2006-02675
                                            A-5                                  Attachment
CR-RBS-2006-02402
CR-RBS-2005-02331


Section 4OA2: Identification and Resolution of Problems
Attachment
A-6
Section 4OA2: Identification and Resolution of Problems
Semiannual Trend Review
Semiannual Trend Review
CR-RBS-2004-02165                 CR-RBS-2006-01270              CR-RBS-2006-02469
CR-RBS-2004-02165
CR-RBS-2006-00159                 CR-RBS-2006-01324              CR-RBS-2006-02484
CR-RBS-2006-00159
CR-RBS-2006-00226                 CR-RBS-2006-01333              CR-RBS-2006-02540
CR-RBS-2006-00226
CR-RBS-2006-00279                 CR-RBS-2006-01429              CR-RBS-2006-02544
CR-RBS-2006-00279
CR-RBS-2006-00296                 CR-RBS-2006-01464              CR-RBS-2006-02550
CR-RBS-2006-00296
CR-RBS-2006-00434                 CR-RBS-2006-01489              CR-RBS-2006-02558
CR-RBS-2006-00434
CR-RBS-2006-00663                 CR-RBS-2006-01490              CR-RBS-2006-02559
CR-RBS-2006-00663
CR-RBS-2006-00798                 CR-RBS-2006-02269              CR-RBS-2006-02651
CR-RBS-2006-00798
CR-RBS-2006-00799                 CR-RBS-2006-02348              CR-RBS-2006-02661
CR-RBS-2006-00799
CR-RBS-2006-00928                 CR-RBS-2006-02349              CR-RBS-2006-02682
CR-RBS-2006-00928
CR-RBS-2006-00993                 CR-RBS-2006-02356              CR-RBS-2006-02683
CR-RBS-2006-00993
CR-RBS-2006-01131                 CR-RBS-2006-02375              CR-RBS-2006-02732
CR-RBS-2006-01131
CR-RBS-2006-01132                 CR-RBS-2006-02406              CR-RBS-2006-02733
CR-RBS-2006-01132
CR-RBS-2006-01205                 CR-RBS-2006-02407              CR-RBS-2006-02799
CR-RBS-2006-01205
CR-RBS-2006-01261
CR-RBS-2006-01261
Section 2OS1: Access Controls to Radiologically Significant Areas
CR-RBS-2006-01270
CR-RBS-2006-01324
CR-RBS-2006-01333
CR-RBS-2006-01429
CR-RBS-2006-01464
CR-RBS-2006-01489
CR-RBS-2006-01490
CR-RBS-2006-02269
CR-RBS-2006-02348
CR-RBS-2006-02349
CR-RBS-2006-02356
CR-RBS-2006-02375
CR-RBS-2006-02406
CR-RBS-2006-02407
CR-RBS-2006-02469
CR-RBS-2006-02484
CR-RBS-2006-02540
CR-RBS-2006-02544
CR-RBS-2006-02550
CR-RBS-2006-02558
CR-RBS-2006-02559
CR-RBS-2006-02651
CR-RBS-2006-02661
CR-RBS-2006-02682
CR-RBS-2006-02683
CR-RBS-2006-02732
CR-RBS-2006-02733
CR-RBS-2006-02799
Section 2OS1: Access Controls to Radiologically Significant Areas  
Corrective Action Documents
Corrective Action Documents
CR-RBS-2006-00090 CR-RBS- 2006-01294 CR-RBS-2006-01787 CR-RBS- 2006-01950
CR-RBS-2006-00090   CR-RBS- 2006-01294   CR-RBS-2006-01787   CR-RBS- 2006-01950
Radiation Work Permits
Radiation Work Permits
2006-1915     RFO-13, Remove and Replace LPRMs, Including Support Activities
2006-1915
2006-1921     RFO-13, Flow Control Valve Maintenance, Including Support Activities
RFO-13, Remove and Replace LPRMs, Including Support Activities
2006-1929     RFO-13, Recirc Pump Work, Including Support Activities
2006-1921
RFO-13, Flow Control Valve Maintenance, Including Support Activities
2006-1929
RFO-13, Recirc Pump Work, Including Support Activities
Procedures
Procedures
RP-103         Access Control, Revision 2
RP-103
RP-106         Radiological Survey Documentation, Revision 1
Access Control, Revision 2
RP-108         Radiation Protection Posting, Revision 2
RP-106
RPP-0006       Performance of Radiological Surveys, Revision 19
Radiological Survey Documentation, Revision 1
Section 2OS2: ALARA Planning and Controls (71121.02)
RP-108
Radiation Protection Posting, Revision 2
RPP-0006
Performance of Radiological Surveys, Revision 19
Section 2OS2: ALARA Planning and Controls (71121.02)
Corrective Action Documents
Corrective Action Documents
CR-RBS-2006-01746
CR-RBS-2006-01746
Procedures
Procedures
ENS-RP-105 Radiation Work Permits, Revision 7
ENS-RP-105 Radiation Work Permits, Revision 7
                                              A-6                                Attachment


                              LIST OF ACRONYMS
Attachment
CDF   core damage frequency
A-7
ALARA as low as is reasonably achievable
LIST OF ACRONYMS
ASME   American Society of Mechanical Engineers
CDF
CAP   corrective action program
core damage frequency
CFR   Code of Federal Regulations
ALARA
CR-RBS River Bend Station condition report
as low as is reasonably achievable
EDG   emergency diesel generator
ASME
LER   licensee event report
American Society of Mechanical Engineers
MC     inspection manual chapter
CAP
NCV   noncited violation
corrective action program
NDE   nondestructive examination
CFR
NEI   Nuclear Energy Institute
Code of Federal Regulations
NRC   U.S. Nuclear Regulatory Commission
CR-RBS
ORAT   outage risk assessment team
River Bend Station condition report
PI     performance indicators
EDG
RCS   reactor coolant system
emergency diesel generator
RFO   refueling outage
LER
SFC   spent fuel pool cooling system
licensee event report
SOP   system operating procedures
MC
SR     surveillance requirement
inspection manual chapter
SSC   structures, systems, or components
NCV
STP   surveillance test procedure
noncited violation
TS     Technical Specifications
NDE
USAR   Updated Safety Analysis Report
nondestructive examination
WO     work order
NEI
WR     work request
Nuclear Energy Institute
                                      A-7      Attachment
NRC
U.S. Nuclear Regulatory Commission
ORAT
outage risk assessment team
PI
performance indicators
RCS
reactor coolant system
RFO
refueling outage
SFC
spent fuel pool cooling system
SOP
system operating procedures
SR
surveillance requirement
SSC
structures, systems, or components
STP
surveillance test procedure
TS
Technical Specifications
USAR
Updated Safety Analysis Report
WO
work order
WR
work request
}}
}}

Latest revision as of 07:23, 15 January 2025

IR 05000458/2006003; 04/01/2006 - 06/30/2006; River Bend Station; Operability Evaluations, Refueling and Other Outage Activities, Surveillance Testing, Occupational Radiation Safety
ML062260238
Person / Time
Site: River Bend Entergy icon.png
Issue date: 08/14/2006
From: Kennedy K
NRC/RGN-IV/DRP/RPB-C
To: Hinnenkamp P
Entergy Operations
References
IR-06-003
Download: ML062260238 (45)


See also: IR 05000458/2006003

Text

August 14, 2006

Paul D. Hinnenkamp

Vice President - Operations

Entergy Operations, Inc.

River Bend Station

5485 US Highway 61N

St. Francisville, LA 70775

SUBJECT:

RIVER BEND STATION - NRC INTEGRATED INSPECTION

REPORT 05000458/2006003

Dear Mr. Hinnenkamp:

On June 30, 2006, the U.S. Nuclear Regulatory Commission (NRC) completed an inspection at

your River Bend Station. The enclosed integrated inspection report documents the inspection

results, which were discussed on July 5, 2006, with you and other members of your staff.

The inspection examined activities conducted under your license as they relate to safety and

compliance with the Commissions rules and regulations and with the conditions of your license.

The inspectors reviewed selected procedures and records, observed activities, and interviewed

personnel.

The report documents three NRC-identified findings and two self-revealing findings of very low

safety significance (Green). The NRC has also determined that violations are associated with

these findings. However, because these violations were of very low safety significance and

were entered into your corrective action program, the NRC is treating these violations as

noncited violations, consistent with Section VI.A.1 of the NRC Enforcement Policy. If you

contest the violations or the significance of the violations, you should provide a response within

30 days of the date of this inspection report, with the basis for your denial, to the U.S. Nuclear

Regulatory Commission, ATTN: document Control Desk, Washington, DC 20555-0001, with

copies to the Regional Administrator, U.S. Nuclear Regulatory Commission, Region IV, 611

Ryan Plaza Drive, Suite 400, Arlington, Texas 76011-4005; the Director, Office of Enforcement,

U.S. Nuclear Regulatory Commission, Washington, DC 20555-0001; and the NRC Resident

Inspector at the River Bend Station facility.

In accordance with 10 CFR 2.390 of the NRCs Rules of Practice, a copy of this letter, its

enclosure, and your response (if any) will be available electronically for public inspection in the

NRC Public Document Room or from the Publicly Available Records (PARS) component of

NRCs document system (ADAMS). ADAMS is accessible from the NRC Website at

http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room).

Entergy Operations, Inc.

-2-

Should you have any questions concerning this inspection, we will be pleased to discuss them

with you.

Sincerely,

/RA/

Kriss M. Kennedy, Chief

Project Branch C

Division of Reactor Projects

Docket: 50-458

License: NPF-47

Enclosure:

NRC Inspection Report 05000458/2006003

w/Attachment: Supplemental Information

cc w/enclosure:

Senior Vice President and

Chief Operating Officer

Entergy Operations, Inc.

P.O. Box 31995

Jackson, MS 39286-1995

Vice President

Operations Support

Entergy Operations, Inc.

P.O. Box 31995

Jackson, MS 39286-1995

General Manager

Plant Operations

Entergy Operations, Inc.

River Bend Station

5485 US Highway 61N

St. Francisville, LA 70775

Director - Nuclear Safety

Entergy Operations, Inc.

River Bend Station

5485 US Highway 61N

St. Francisville, LA 70775

Wise, Carter, Child & Caraway

P.O. Box 651

Jackson, MS 39205

Entergy Operations, Inc.

-3-

Winston & Strawn LLP

1700 K Street, N.W.

Washington, DC 20006-3817

Manager - Licensing

Entergy Operations, Inc.

River Bend Station

5485 US Highway 61N

St. Francisville, LA 70775

The Honorable Charles C. Foti, Jr.

Attorney General

Department of Justice

State of Louisiana

P.O. Box 94005

Baton Rouge, LA 70804-9005

H. Anne Plettinger

3456 Villa Rose Drive

Baton Rouge, LA 70806

Bert Babers, President

West Feliciana Parish Police Jury

P.O. Box 1921

St. Francisville, LA 70775

Richard Penrod, Senior Environmental

Scientist

Office of Environmental Services

Northwestern State University

Russell Hall, Room 201

Natchitoches, LA 71497

Brian Almon

Public Utility Commission

William B. Travis Building

P.O. Box 13326

1701 North Congress Avenue

Austin, TX 78711-3326

Entergy Operations, Inc.

-4-

Chairperson

Denton Field Office

Chemical and Nuclear Preparedness

and Protection Division

Office of Infrastructure Protection

Preparedness Directorate

Dept. of Homeland Security

800 North Loop 288

Federal Regional Center

Denton, TX 76201-3698

Entergy Operations, Inc.

-5-

Electronic distribution by RIV:

Regional Administrator (BSM1)

DRP Director (ATH)

DRS Director (DDC)

DRS Deputy Director (RJC1)

Senior Resident Inspector (PJA)

Branch Chief, DRP/C (KMK)

Senior Project Engineer, DRP/C (WCW)

Team Leader, DRP/TSS (RLN1)

RITS Coordinator (KEG)

DRS STA (DAP)

J. Lamb, OEDO RIV Coordinator (JGL1)

ROPreports

RBS Site Secretary (LGD)

W. A. Maier, RSLO (WAM)

SUNSI Review Completed: __wcw_ ADAMS:  : Yes

G No Initials: __wcw___

Publicly Available G Non-Publicly Available G Sensitive
Non-Sensitive

R:\\_REACTORS\\_RB\\2006\\RB2006-03RP-PJA.wpd

RIV:SRI:DRP/C

RI:DRP/C

C:DRS/OB

C:DRS/EB1

C:DRS/PSB

PJAlter

MOMiller

ATGody

JAClark

MPShannon

T - WCWalker

E - WCWalker

/RA/

/RA/

/RA/

8/10/06

8/10/06

8/11/06

8/10/06

8/10/06

C:DRS/EB2

SRA:DRS

C:DRP/C

LJSmith

DPLoveless

KMKennedy

/RA/

/RA/

/RA/

8/10/06

8/14/06

8/14/06

OFFICIAL RECORD COPY

T=Telephone E=E-mail F=Fax

Enclosure

-1-

U.S. NUCLEAR REGULATORY COMMISSION

REGION IV

Docket:

50-458

License:

NPF-47

Report:

05000458/2006003

Licensee:

Entergy Operations, Inc.

Facility:

River Bend Station

Location:

5485 U.S. Highway 61

St. Francisville, Louisiana

Dates:

April 1 to June 30, 2006

Inspectors:

P. Alter, Senior Resident Inspector, Project Branch C

M. Miller, Resident Inspector, Project Branch C

G. Werner, Senior Project Engineer, Project Branch D

L. Ricketson, P.E., Senior Health Physicist, Plant Support Branch

W. Sifre, Senior Reactor Inspector, Engineering Branch 1

Approved By:

Kriss M. Kennedy, Chief

Project Branch C

Division of Reactor Projects

Enclosure

-2-

TABLE OF CONTENTS

SUMMARY OF FINDINGS . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 3

REPORT DETAILS . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 6

REACTOR SAFETY . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 6

1R01

Adverse Weather Protection . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 6

1R04

Equipment Alignment . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 7

1R05

Fire Protection . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 7

1R08

Inservice Inspection Activities . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 8

1R11

Licensed Operator Requalification Program . . . . . . . . . . . . . . . . . . . . . . . . . . . 9

1R12

Maintenance Effectiveness . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 10

1R13

Maintenance Risk Assessments and Emergent Work Control . . . . . . . . . . . . . 10

1R14

Operator Performance During Nonroutine Evolutions and Events . . . . . . . . . . 11

1R15

Operability Evaluations . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 12

1R19

Postmaintenance Testing . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 17

1R20

Refueling and Other Outage Activities . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 17

1R22

Surveillance Testing

. . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 20

1R23

Temporary Plant Modifications

. . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 23

1EP6 Drill Evaluation . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 23

RADIATION SAFETY . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 24

2OS1 Access Control to Radiologically Significant Areas . . . . . . . . . . . . . . . . . . . . . 24

2OS2 ALARA Planning and Controls . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 27

OTHER ACTIVITIES . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 28

4OA1 Performance Indicator (PI) Verification . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 28

4OA2 Identification and Resolution of Problems . . . . . . . . . . . . . . . . . . . . . . . . . . . . 29

4OA3 Event Followup . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 31

4OA5 Other Activities . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 32

4OA6 Meetings, Including Exit . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 32

SUPPLEMENTAL INFORMATION . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . A-1

KEY POINTS OF CONTACT . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . A-1

LIST OF ITEMS OPENED, CLOSED, AND DISCUSSED . . . . . . . . . . . . . . . . . . . . . . . . . . . A-1

LIST OF DOCUMENTS REVIEWED . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . A-2

LIST OF ACRONYMS . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . A-7

Enclosure

-3-

SUMMARY OF FINDINGS

IR 05000458/2006003; 04/01/2006 - 06/30/2006; River Bend Station; Operability Evaluations,

Refueling and Other Outage Activities, Surveillance Testing, Occupational Radiation Safety.

The report covered a 3-month period of routine baseline inspections by resident inspectors and

announced baseline inspections by regional engineering and radiation protection inspectors.

Five Green noncited violations were identified. The significance of most findings is indicated by

their color (Green, White, Yellow, Red) using Inspection Manual Chapter 0609, Significance

Determination Process. Findings for which the significance determination process does not

apply may be Green or be assigned a severity level after NRC management review. The

NRCs program for overseeing the safe operation of commercial nuclear power reactors is

described in NUREG-1649, Reactor Oversight Process, Revision 3, dated July 2000.

A.

NRC-Identified and Self-Revealing Findings

Cornerstone: Mitigating Systems

Green. A self-revealing noncited violation of 10 CFR Part 50, Appendix B, Criterion XVI,

"Corrective Action," was reviewed involving the failure of the licensee to identify that the

normal supply breaker to the Division III 4.16 kV engineered safety features bus was not

properly racked in for a period of 24 days following maintenance. This issue was

entered into the licensee's corrective action program as CR-RBS-2006-02402.

The finding was more than minor because it was associated with the mitigating system

cornerstone attribute of configuration control and affected the associated cornerstone

objective to ensure the availability, reliability, and capability of systems that respond to

initiating events to prevent undesirable consequences. Utilizing Manual Chapter 0609,

"Significance Determination Process," a Phase 3 analysis concluded that the finding

was of very low safety significance. The cause of the finding was related to the

crosscutting aspect of problem identification and resolution in that the licensee failed to

properly evaluate available indications to identify that the breaker was not properly

racked in. (Section 1R15).

Green. An NRC identified noncited violation of 10 CFR 50.65 Maintenance Rule

Section (a)(4) was identified for the failure of the licensee to provide prescribed

compensatory measures for two Orange shutdown risk conditions during Refueling

Outage 13. Specifically, the preoutage risk assessment recommended that two work

orders be in place for maintenance electricians to provide power to one spent fuel pool

cooling pump in the event of problems with the running pump during periods of electrical

bus maintenance. The inspectors found that the work packages were not in place

before entering shutdown risk condition Orange on April 26, 2006, during the Division II

engineering safety features bus testing, and May 3, 2006, during the Division I

engineered safety features bus outage. This issue was entered into the licensee's

corrective action program as CR-RBS-2006-01937.

The finding was more than minor because the licensee failed to implement a prescribed

compensatory measure during the highest risk condition of Refueling Outage 13. The

Enclosure

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specific compensatory measures were called for in the preoutage risk assessment and

the shutdown operations protection plan. The finding affected the mitigating system

cornerstone because of the increased risk of a sustained loss of spent fuel pool cooling

during core offloading operations. The finding could not be evaluated using the

significance determination process, therefore the finding was reviewed by regional

management and determined to be of very low safety significance. Factors that were

considered included: (1) electrical maintenance technicians had previously performed

the task of providing alternate power to a spent fuel pool cooling pump, (2) the

necessary equipment was staged as part of the abnormal operating procedure for loss

of decay heat removal, and (3) the relatively long time to boil of the spent fuel storage

pool at that time during the refueling outage. The cause of the finding was related to the

crosscutting aspect of human performance because the licensees planned

maintenance activities and the predetermined increase in outage risk was not effectively

managed by prescribed compensatory measures (Section 1R20).

Green. An NRC identified noncited violation of Technical Specification 5.4.1.a was

identified for the failure of the licensee to provide an adequate surveillance test

procedure to perform Technical Specification Surveillance Requirement 3.8.1.1.

Specifically, STP-000-0102, Power Distribution Alignment Check, Revision 4, did not

verify the required offsite power circuit breaker alignment and indicated power

availability for the Division III 4.16 kV engineered safety features bus as required in

Modes 1, 2, and 3. This issue was entered into the licensee's corrective action program

as CR-RBS-2006-02675 and -02402.

The finding was more than minor because it was associated with the mitigating system

cornerstone attribute of configuration control and affected the associated cornerstone

objective to ensure the availability, reliability, and capability of systems that respond to

initiating events to prevent undesirable consequences. Utilizing Manual Chapter 0609,

"Significance Determination Process," a Phase 3 analysis concluded that the finding

was of very low safety significance. (Section 1R22).

Cornerstone: Occupational Radiation Safety

Green. The inspector reviewed a self-revealing noncited violation of Technical Specification 5.7.1, resulting from the licensees failure to control access to a high

radiation area. While transferring reverse osmosis system filters in the radwaste

building, the licensee allowed two workers to inadvertently enter a high radiation area.

This occurred after a guard prematurely left his post in front of the 123 foot elevation

elevator door. The highest dose rate recorded by an electronic alarming dosimeter was

164 millirem per hour. The guard returned and evacuated the workers before they

accrued additional radiation dose. Planned corrective action was still being evaluated by

the licensee at the conclusion of the inspection.

The finding was more than minor because it was associated with the occupational

radiation safety attribute of exposure control and affected the cornerstone objective in

that not controlling a high radiation area could increase personal exposure. Using the

Occupational Radiation Safety Significance Determination Process, the inspector

determined that the finding was of very low safety significance because it did not

Enclosure

-5-

involve: (1) an as low as is reasonably achievable finding, (2) an overexposure, (3) a

substantial potential for overexposure, or (4) an impaired ability to assess dose.

Additionally, this finding had crosscutting aspects associated with human performance

in that the failure of the individual to guard the elevator door directly contributed to the

violation. (Section 2OS1)

Green. The inspector identified a noncited violation of 10 CFR 20.1501(a) because the

license failed to survey airborne radioactivity. During the removal of local power range

monitors, the licensee started collecting an air sample of the work area, but discarded

the sample before analyzing it. Successful passage through the portal monitors at the

exit of the controlled access area confirmed that no worker experienced an uptake of

radioactive material. Planned corrective action is still being evaluated.

The finding was more than minor because it was associated with the occupational

radiation safety program attribute of exposure control and affected the cornerstone

objective in that the lack of knowledge of radiological conditions could increase

personnel dose. Using the Occupational Radiation Safety Significance Determination

Process, the inspector determined that the finding was of very low safety significance

because it did not involve: (1) an as low as is reasonably achievable finding, (2) an

overexposure, (3) a substantial potential for overexposure, or (4) an impaired ability to

assess dose. Additionally, this finding had crosscutting aspects associated with human

performance in that the failure to maintain the sample for analysis directly contributed to

the violation. (Section 2OS1)

B.

Licensee-Identified Violations

None.

Enclosure

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REPORT DETAILS

Summary of Plant Status: The reactor was operated at 100 percent power from April 1-15,

2006, when the reactor scrammed due to a control circuit failure which caused both reactor

recirculation pumps to shift to slow speed. The reactor was restarted on April 17 and attained

100 percent power on April 18. On April 23, the reactor was shut down for Refueling Outage

(RFO) -13. On May 12, the reactor was restarted and attained 100 percent power on May 18.

On June 15, reactor power was reduced to 23 percent because of a problem with the main

turbine bypass valves. The reactor was returned to 100 percent power on June 18. The

reactor remained at 100 percent power for the remainder of the inspection period, with the

exception of regularly scheduled power reductions for control rod pattern adjustments and

turbine testing.

1.

REACTOR SAFETY

Cornerstones: Initiating Events, Mitigating Systems, Barrier Integrity, Emergency

Preparedness

1R01

Adverse Weather Protection

a.

Inspection Scope

Hurricane Season Preparations

During the week of June 12, 2006, the inspectors completed a review of the licensee's

readiness for seasonal susceptibilities involving high winds at the beginning of hurricane

season. The inspectors reviewed Procedure ENS-EP-302, Severe Weather

Response, Revision 4. The inspectors: (1) reviewed plant procedures, the Updated

Safety Analysis Report (USAR), and Technical Specifications (TS) to verify that operator

actions defined in adverse weather procedures maintained the readiness of essential

systems; (2) walked down portions of the protected area to verify that hurricane season

preparations were sufficient to support operability of essential systems, including the

ability to perform safe shutdown functions; (3) evaluated operator staffing levels to verify

the licensee could maintain the readiness of essential systems required by plant

procedures; and (4) reviewed the corrective action program (CAP) to determine if the

licensee identified and corrected problems related to adverse weather conditions.

The inspectors completed one inspection sample.

b.

Findings

No findings of significance were identified.

Enclosure

-7-

1R04

Equipment Alignment

Partial System Walkdowns

a.

Inspection Scope

The inspectors: (1) walked down portions of the three risk important systems listed

below and reviewed system operating procedures (SOPs), piping and instrument

diagrams, and other documents to verify that critical portions of the selected systems

were correctly aligned; and (2) compared deficiencies identified during the walkdown to

the licensee's USAR and CAP to verify problems were being identified and corrected.

Alternate decay heat removal system, which was the backup to the inservice

shutdown cooling system during refueling operations, on May 2, 2006

Reactor core isolation cooling system, while the high pressure core spray diesel

was out of service for maintenance, on June 12, 2006

Division I emergency diesel generator (EDG), while Division II EDG was out of

service for planned maintenance, on June 21, 2006

Documents reviewed by the inspectors included:

SOP-0140, Suppression Pool Cleanup and Alternate Decay Heat Removal,

Revision 16

SOP-0035, Reactor Core Isolation Cooling System, Revision 8A

SOP-0053, Standby Diesel Generator and Auxiliaries, Revision 44A

The inspectors completed three inspection samples.

h.

Findings

No findings of significance were identified.

1R05

Fire Protection

b.

Inspection Scope

The inspectors walked down the six plant areas listed below to assess the material

condition of active and passive fire protection features and their operational lineup and

readiness. The inspectors: (1) verified that transient combustibles were controlled in

accordance with plant procedures; (2) observed the condition of fire detection devices to

verify they remained functional; (3) observed fire suppression systems to verify they

remained functional and that access to manual actuators was unobstructed; (4) verified

that fire extinguishers and hose stations were provided at their designated locations and

Enclosure

-8-

that they were in a satisfactory condition; (5) verified that passive fire protection features

(electrical raceway barriers, fire doors, fire dampers, steel fire proofing, penetration

seals, and oil collection systems) were in a satisfactory material condition; (6) verified

that adequate compensatory measures were established for degraded or inoperable fire

protection features and that the compensatory measures were commensurate with the

significance of the deficiency; and (7) reviewed the CAP to determine if the licensee

identified and corrected fire protection problems.

Auxiliary building piping Tunnel D, Fire Area AB-7, on May 9, 2006

Low pressure core spray pump room, Fire Area AB-6/Z-1, on May 9, 2006

High pressure core spray pump room, Fire Area AB-2/Z-1, on May 9, 2006

Control building standby switchgear Room 1A, Fire Area C-15, on June 22, 2006

Control building safety related cable tray area and stairway Number 3, Fire Area

C-16 and C-29, on June 22, 2006

Division I EDG control and diesel engine rooms, Fire Area DG-6/Z-1, on June 22,

2006

Documents reviewed by the inspectors included:

Pre-Fire Plan/Strategy Book

USAR Section 9A.2, Fire Hazards Analysis, Revision 10

River Bend Station postfire safe shutdown analysis

RBNP-038, Site Fire Protection Program, Revision 6B

The inspectors completed six inspection samples.

b.

Findings

No findings of significance were identified.

1R08

Inservice Inspection Activities

a.

Inspection Scope

The inspector witnessed the performance of 12 volumetric (ultrasonic) and four surface

(liquid penetrant) examinations. The sample of nondestructive examination (NDE)

activities is listed in the attachment.

For each of the NDE activities reviewed, the inspector verified that the examinations

were performed in accordance with American Society of Mechanical Engineers (ASME)

Code requirements.

Enclosure

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During the review of each examination, the inspector verified that appropriate NDE

procedures were used, that examinations and conditions were as specified in the

procedure, and that test instrumentation or equipment was properly calibrated and within

the allowable calibration period. The inspector also reviewed documentation to verify

that indications revealed by the examinations were dispositioned in accordance with the

ASME Code specified acceptance standards.

The inspector verified the certifications of the NDE personnel observed performing

examinations or identified during review of completed examination packages.

The inspection procedure requires review of one or two examinations from the previous

outage with recordable indications that were accepted for continued service to ensure

that the disposition was done in accordance with the ASME Code. There were no

recordable indications that required evaluation during the last outage.

If the licensee completed welding on the pressure boundary for Class 1 or 2 systems

since the beginning of the previous outage, the procedure requires verification that

acceptance and preservice examinations were done in accordance with the ASME Code

for one to three welds. There were no welds available for review.

The procedure also requires verification that one or two ASME Code Section XI repairs

or replacements meet code requirements. There were no code repairs or replacements

available at the time of this inspection.

The inspectors completed 16 inspection samples.

b.

Findings

No findings of significance were identified.

1R11

Licensed Operator Requalification Program

a.

Inspection Scope

On June 13, 2006, the inspectors observed testing and training of senior reactor

operators and reactor operators to verify the adequacy of training, to assess operator

performance, and to assess the evaluators critique. The training evaluation scenario

observed was RSMS-OPS-422, Loss of Circ Water Pump, Failure of Steam Flow

Transmitter and Instrument Air System Leak, Revision 4.

The inspectors completed one inspection sample.

b.

Findings

No findings of significance were identified.

Enclosure

-10-

1R12

Maintenance Effectiveness

a.

Inspection Scope

The inspectors reviewed the condition reports (CR) listed below which documented

equipment problems to: (1) verify the appropriate handling of structure, system, and

component (SSC) performance or condition problems; (2) verify the appropriate

handling of degraded SSC functional performance; (3) evaluate the role of work

practices and common cause problems; and (4) evaluate the handling of SSC issues

reviewed under the requirements of the maintenance rule; 10 CFR Part 50, Appendix B;

and TS.

CR-RBS-2006-1898, main steam stop Valve B21-MOVF098C leakage, reviewed

on June 2, 2006, and CR-RBS-2004-4338, main steam stop Valve B21-

MOVF098C high leakage during RFO-11 and -12, reviewed on June 26, 2006.

CR-RBS-2006-2302, primary containment integrity maintenance rule repetitive

functional failure, reviewed on June 26, 2006.

Documents reviewed by the inspectors included:

NUMARC 93-01, Nuclear Energy Institute Industry (NEI) Guideline for Monitoring

the Effectiveness of Maintenance at Nuclear Power Plants, Revision 2

Maintenance rule function list

Maintenance rule performance criteria list

Main steam stop valve maintenance rule performance evaluations

The inspectors completed two inspection samples.

b.

Findings

No findings of significance were identified.

1R13

Maintenance Risk Assessments and Emergent Work Control

a.

Inspection Scope

.1

Risk Assessment and Management of Risk

The inspectors reviewed the planned work weeks listed below to verify: (1) that the

licensee performed risk assessments when required by 10 CFR 50.65 (a)(4) and

administrative Procedure ADM-096, Risk Management Program Implementation and

On-Line Maintenance Risk Assessment, Revision 4B, prior to changes in plant

configuration for maintenance activities and plant operations; (2) the accuracy,

adequacy, and completeness of the information considered in the risk assessment;

Enclosure

-11-

(3) that the licensee recognized, and entered as applicable, the appropriate licensee

established risk category according to the risk assessment results and Procedure ADM-

096; and (4) that the licensee identified and corrected problems related to maintenance

risk assessments. Specific work activities evaluated included planned and emergent

work for the weeks of:

June 5, 2006, Division I work week and preferred station service Transformer

RTX-ESR1F cooling oil dehydration

June 19, 2006, planned Division II EDG outage week

June 26, 2006, nondivisional work week and potential labor work stoppage

.2

Emergent Work Control

For the two emergent work activities listed below, the inspectors: (1) verified that the

licensee performed actions to minimize the probability of initiating events and

maintained the functional capability of mitigating systems and barrier integrity systems;

(2) verified that emergent work related activities such as troubleshooting, work

planning/scheduling, establishing plant conditions, aligning equipment, tagging,

temporary modifications, and equipment restoration did not place the plant in an

unacceptable configuration; and (3) reviewed the CAP to determine if the licensee

identified and corrected risk assessment and emergent work control problems.

Preferred station service Transformer RTX-ESR1F sudden pressure relay failure

on May 30, 2006

Main turbine bypass valves inoperable due to hydraulic oil leak on June 2, 2006

The inspectors completed five inspection samples.

c.

Findings

No findings of significance were identified.

1R14

Operator Performance During Nonroutine Evolutions and Events

a.

Inspection Scope

1.

April 4, 2006, Automatic Initiation of Standby Service Water

The inspectors: (1) reviewed operator logs, plant computer data, and strip charts for the

April 4, 2006, unexpected initiation of Division II standby service water that occurred

while swapping the running normal service water pumps to evaluate operator

performance in coping with the event; (2) verified that operator actions were in

accordance with the response required by plant procedures and training; and (3) verified

that the licensee identified and implemented appropriate corrective actions associated

with personnel performance problems that occurred during the transient. In addition, the

Enclosure

-12-

inspectors reviewed CR-RBS-2006-01257, which documented the procedural problems

that led to the event and reviewed the following procedures used by the operators:

AOP-53, Initiation of Standby Service Water With Normal Service Water

Running, Revision 8

SOP-42, Standby Service Water System, Revision 25

SOP-66, Control Building HVAC Chilled Water System, Revision 33B

2.

April 15, 2006, Reactor Scram

The inspectors: (1) reviewed operator logs, plant computer data, and strip charts for the

April 15, 2006, unexpected reactor recirculation pump downshift and subsequent reactor

scram to evaluate operator performance in coping with the event; (2) verified that

operator actions were in accordance with the response required by plant procedures

and training; and (3) verified that the licensee identified and implemented appropriate

corrective actions associated with personnel performance problems that occurred during

the transient. In addition the inspectors reviewed the postscram report documented in

Procedure GOP-003, Scram Recovery, Revision 16A, and observed the onsite safety

review committee review of the postscram report.

The inspectors completed two inspection samples.

e.

Findings

No findings of significance were identified.

1R15

Operability Evaluations

a.

Inspection Scope

For the operability evaluations associated with the documents listed below, the

inspectors: (1) reviewed plants status documents such as operator shift logs, emergent

work documentation, deferred modifications, and standing orders, to determine if an

operability evaluation was warranted for degraded components; (2) referred to the

USAR and design basis documents to review the technical adequacy of licensee

operability evaluations; (3) evaluated compensatory measures associated with

operability evaluations; (4) determined degraded component impact on any TS; (5) used

the significance determination process to evaluate the risk significance of degraded or

inoperable equipment; and (6) verified that the licensee identified and implemented

appropriate corrective actions associated with degraded components.

CR-RBS-2006-01207 and -01215, Primary containment purge exhaust line fails

to meet leak rate acceptance criteria, reviewed during the week of April 3, 2006

Enclosure

-13-

CR-RBS-2005-02805, Inserted control Rod 24-29 control blade lifetime

calculation revised for extended operating cycle, reviewed during the week of

April 17, 2006

Work Request (WR) 76625, NNS-ACB23 control power light out, suspect bad

socket, reviewed during the week of May 29, 2006

TS-LCO-06-0711, Division II EDG Generator Output Breaker charging springs

did not charge during tagout restoration, reviewed on June 23, 2006

CR-RBS-2006-01257, Division II standby service water start on low service water

pressure, reviewed on June 28, 2006

CR-RBS-2006-02632, turbine bypass valves hydraulic oil leak, reviewed on

June 28, 2006

Other documents reviewed by the inspectors are listed in the attachment.

The inspectors completed six inspection samples.

b.

Findings

Introduction: The inspectors reviewed a self-revealing noncited violation (NCV) of

10 CFR Part 50, Appendix B, Criterion XVI, "Corrective Action," involving the failure of

the licensee to identify that the normal supply breaker to the Division III 4.16 kV

engineered safety features (ESF) bus was not properly racked in following maintenance.

Description: Following the completion of planned maintenance on Switchgear NNS-

SWG1A on April 29, 2006, operators were assigned to clear equipment tags and restore

the system alignment. As part of this task, operators racked in Breaker NNS-ACB23,

the normal supply breaker to 4.16 kV Switchgear NNS-SWG1C. No actions, such as

cycling the breaker, were required to verify that the breaker was properly racked in.

On May 9, 2006, after noting that the control power light associated with Breaker NNS-

ACB23 was not lit, operators wrote WR 76625 to repair the light. The WR stated that

the white control power light on Control Room Panel H13-P808 was out with the breaker

racked in and the control power fuses installed. The WR also indicated that the

suspected cause was a bad socket and that position Switch 52H had failed in the past to

make up during closure. A work control center senior reactor operator determined that

an operability evaluation was not required for the condition described in WR 76625. The

WR was classified 4D, which indicated that it should be scheduled as resources

allowed within the normal 16-week work planning schedule. The inspectors noted the

licensee did not write a CR. The white control power light provides indication that the

breaker is functional, specifically, that: (1) there is no electrical fault on the line or load

side of the breaker, (2) the breaker Lockout button is not depressed on Panel 808, and

(3) the breaker is fully racked into the switchgear. On May 9, 2006, there were no

electrical faults on Breaker NNS-ACB23 and the Lockout was reset on Panel 808.

Enclosure

-14-

On May 22, 2006, while aligning Switchgear NNS-SWG1C and the Division III 4.16 kV

ESF bus to the Transformer RSS1 offsite power supply, Breaker NNS-ACB23 failed to

close. Operators racked the breaker out and in, but the breaker failed to close on the

second attempt. Subsequent troubleshooting identified that the breaker had not been

fully racked in as electricians were able to rotate the racking device one additional turn.

The white light on Panel 808 came on and the breaker was successfully closed. The

operators and electricians determined that Breaker NNS-ACB23 had not been not

properly racked in, wrote CR-RBS-2006-02325 and -02337 and initiated WR 77478 to

investigate the problem with racking in Breaker NNS-ACB23.

On May 25, 2006, the inspectors questioned the impact that the failure of the breaker to

close had on the licensees compliance with TS. Specifically, TS 3.8.1.a requires two

qualified circuits between the offsite transmission network and the onsite Class 1E ac

electrical power distribution system when the plant is in Modes 1, 2, and 3. On May 12,

the plant was taken from Mode 4 to Mode 2 without two qualified offsite power sources

available to the Division III 4.16 kV ESF bus. The licensee wrote CR-RBS-2006-2402

and determined that they did not comply with TS 3.8.1.a when they changed modes on

May 12. In addition, the Division III 4.16 kV ESF bus was inoperable for a period of

10 days (May 12-22), which exceeded the allowed outage time of 72 hours8.333333e-4 days <br />0.02 hours <br />1.190476e-4 weeks <br />2.7396e-5 months <br /> specified in

TS Condition 3.8.1.A. The licensee also discovered that, on May 14 during the conduct

of maintenance on the Division I EDG, with Breaker NNS-ACB23 unable to be closed,

they unknowingly entered TS Condition 3.8.1.d. TS Condition 3.8.1.d states that with

One required offsite circuit inoperable AND on required [E]DG inoperable, restore the

EDG or the offsite power supply to an operable status in 12 hours1.388889e-4 days <br />0.00333 hours <br />1.984127e-5 weeks <br />4.566e-6 months <br /> or place the plant in

Mode 3 within the next 12 hours1.388889e-4 days <br />0.00333 hours <br />1.984127e-5 weeks <br />4.566e-6 months <br />. The Division I EDG was inoperable for 15 hours1.736111e-4 days <br />0.00417 hours <br />2.480159e-5 weeks <br />5.7075e-6 months <br /> and

15 minutes.

The inspectors found that the licensees procedures did not require Breaker NNS-

ACB23 to be cycled to verify proper operation after it was racked in on April 29.

Procedure OSP-0022, Operations General Administrative Guidelines, Revision 01,

step 4.5.5, required that breakers be functionally tested following any activity involving

safety related equipment which requires the breaker to be racked out. Because

Breaker NNS-ACB23 is not classified as a safety-related breaker, it was not required to

be functionally tested after it was racked in on April 29.

Analysis: The performance deficiency associated with this finding involved the failure of

operators to identify that Breaker NNS-ACB23 was not functional on April 29, 2006. The

finding was more than minor because it was associated with the mitigating system

cornerstone attribute of configuration control and affected the associated cornerstone

objective to ensure the availability, reliability, and capability of systems that respond to

initiating events to prevent undesirable consequences. The Phase 1 worksheets in

Manual Chapter (MC) 0609, "Significance Determination Process," were used to

conclude that a Phase 2 analysis was required because both the mitigating systems and

the containment barrier cornerstones were affected.

In accordance with NRC Inspection Manual Chapter 0609, Appendix A, Attachment 1,

"User Guidance for Determining the Significance of Reactor Inspection Findings for

At-Power Situations," the inspectors estimated the risk of the subject finding using the

Enclosure

-15-

Risk-Informed Inspection Notebook for River Bend Station, Revision 2. The inspectors

assumed that Division III power was available, but degraded, while Breaker NNS-ACB23

was not properly installed for the 10 days that the plant was in Mode 3 or above, from

May 12-22, 2006. Therefore, the exposure window used was 3-30 days. No operator

recovery was credited because on two occasions, operators had proven incapable of

properly positioning the breaker, ultimately requiring maintenance technicians to

properly install the breaker. Using Manual Chapter 0609, Appendix A, Attachment 2,

Rule 2.1, Inspection Finding that Degrades Mitigation Capability and Does Not Reduce

Remaining Mitigation Capability Credit to a Value Less Than Full Mitigation Credit, the

inspectors determined that all sequences containing the functions that would be affected

by a loss of Division III power, including the Division I standby service water loop

(HPCS, LPI, CHR, HPCS/LC, and REC/SSW), should be quantified, giving full mitigation

capability credit to each of these functions. Because the performance deficiency

affected the electric power system, Table 2 of the risk-informed notebook required that

all worksheets be evaluated. The resulting dominant sequences are provided in Table 1

below:

Table 1

Phase 2 Worksheet Results

Initiator

Sequence

IEL

Mitigating Functions

Result

TNSW

5

3

SSW - REC/SSW

7*

4

3

RCIC - HPCS - DEP

9*

LOOP

1

3

CHR - LDEP

8

2

3

CHR - SPCFAN

8

4

3

RCIC - HPCS - DEP

9*

6

3

EAC1&2 - HPCS - REC6 - FPW

9*

8

3

EAC1&2 - HPCS - SBODG - REC4

9*

9

3

EAC1&2 - REC1 - HPCS -RCIC

9*

SORV

1

3

CHR-LDEP

8

2

3

CHR - SPCFAN

9

4

3

RCIC - HPCS - DEP

9*

LOIA

2

4

CHR - SPCFAN

8

1

4

CHR-LDEP

9

TPCS

4

2

RCIC - HPCS - DEP

8

ATWS

1

6

CHR

9

  • Denotes sequences indicated as LERF contributors in the Phase 2 notebook.

By application of the counting rule, the internal event risk contribution of this finding to

the change in core damage frequency (CDF) was determined to be of low to moderate

risk significance (WHITE).

A senior reactor analyst performed further evaluation of the risk associated with this

issue (Phase 3/Modified Phase 2). Because the assumptions made during the Phase 2

estimation process were overly conservative and did not completely represent the actual

exposure time nor the actual affect the performance deficiency had on the availability of

power to the Division III diesel generator, the senior reactor analyst modified these

Enclosure

-16-

assumptions to more precisely quantify the change in risk. Specifically, the exposure

time was 10 days as opposed to the 30 days used in the risk-informed notebook.

Additionally, the Phase 2 evaluation included loss of offsite power initiating events that

were not affected by the performance deficiency because offsite power to Division III

would in all likelihood be lost during a design basis loss of offsite power. The senior

reactor analyst performed a modified Phase 2 estimation and determined that the

internal event risk contribution of the subject finding to the CDF was of very low risk

significance (Green). The best estimate value of this probability (CDFINTERNAL) was

calculated by the senior reactor analyst to be 1.2 x 10-7. The analyst evaluated the

contribution of external initiating events to the risk and calculated a bounding risk

estimate of 2.9 x 10-7 as the CDF for internal fire events.

Using Manual Chapter 0609, Appendix H, Containment Integrity Significance

Determination Process, the analyst estimated that the potential risk contribution from

large early release frequency was 6.6 x 10-8.

Given the independence of each initiating event, the analyst determined that the best

estimate of the total risk related to the subject performance deficiency was the

summation of the CDF calculated for both internal and external initiators. Therefore,

the best estimate was 4.1 x 10-7. The change in risk related to large early release

frequency was determined to be below 6.6 x 10-8, corroborating that the finding was of

very low risk significance. The performance deficiency resulted in a finding that was of

very low risk significance (Green). The cause of the finding was related to the

crosscutting aspect of problem identification and resolution in that operators failed to

identify that Breaker NNS-ACB23 was not properly racked in.

Enforcement: 10 CFR Part 50, Appendix B, Criterion XVI, Corrective Action, requires, in

part, that measures be established to assure that conditions adverse to quality are

promptly identified and corrected. Contrary to this, from April 29 to May 22, 2006, the

licensee failed to identify that Breaker NNS-ACB23, which supplied one of the two

required offsite power supplies to the Division III 4.16 kV ESF bus, was not properly

racked in to Switchgear NNS-SWGIC. The root cause involved the licensees lack of

understanding that Breaker NNS-ACB23 was required to be functional to meet

TS 3.8.1.a requirements for two offsite power circuits to the Division III 4.16 kV ESF

bus. The corrective actions to restore compliance included: (1) changes to operations

section procedures to verify the white control power light, when applicable, after a circuit

breaker is racked in, (2) expansion of the requirement to functionally test safety-related

breakers to the nonsafety-related breakers in the TS required offsite power circuits, and

(3) operator lessons learned training on the event and all of its ramifications. Because

the finding was of very low safety significance and has been entered into the licensees

CAP as CR-RBS-2006-02402, this violation is being treated as an NCV consistent with

Section VI.A of the Enforcement Policy: NCV 05000458/2006003-01, Failure to identify

Division III ESF bus supply breaker not racked in.

Enclosure

-17-

1R19

Postmaintenance Testing

a.

Inspection Scope

For the five postmaintenance test activities of risk significant systems or components

listed below, the inspectors: (1) reviewed the applicable licensing basis and/or design-

basis documents to determine the safety functions; (2) evaluated the safety functions

that may have been affected by the maintenance activity; and (3) reviewed the test

procedure to verify that it adequately tested the safety function that may have been

affected. The inspectors either witnessed or reviewed test data to verify that

acceptance criteria were met, plant impacts were evaluated, test equipment was

calibrated, procedures were followed, jumpers were properly controlled, the test data

results were complete and accurate, the test equipment was removed, the system was

properly re-aligned, and deficiencies during testing were documented. The inspectors

also reviewed the CAP to determine if the licensee identified and corrected problems

related to postmaintenance testing.

Work Order (WO) 50370422, Division II battery cell post seal replacement,

reviewed during the week of May 8, 2006

WO 87721, replace control Rods 40-37, 44-41, and 48-25 and 12-25 individual

scram test switches, reviewed May 19, 2006

WO 69816, low pressure core spray keep fill pump discharge check valve, E21-

VF033 replacement, reviewed during the week of June 19, 2006

WO 85194, signature testing on high pressure core spray room unit cooler

service water outlet valve, SWP-MOV74B, reviewed during the week of June 19,

2006

WO 90342, Division II EDG generator output Breaker ENS-SWG1B-ACB027

charging springs failed to charge during tagout restoration, reviewed on June 23,

2006

The inspectors completed five inspection samples.

g.

Findings

No findings of significance were identified.

1R20

Refueling and Other Outage Activities

a.

Inspection Scope

The inspectors reviewed the following risk important refueling outage activities to verify

defense in depth commensurate with the outage risk control plan and compliance with

the TS during RFO-13 from April 23 to May 12, 2006: (1) the risk control plan;

(2) tagging/clearance activities; (3) reactor coolant system instrumentation; (4) electrical

Enclosure

-18-

power; (5) decay heat removal; (6) spent fuel pool cooling; (7) inventory control;

(8) reactivity control; (9) containment closure; (10) reduced inventory conditions;

(11) refueling activities; (12) heatup and cooldown activities; (13) restart activities; and

(14) licensee identification and implementation of appropriate corrective actions

associated with RFO activities. The inspectors' containment inspections included

observations of the containment sump for damage and debris, and supports, braces,

and snubbers for evidence of excessive stress, water hammer, or aging. Specific

outage activities observed and reviewed included:

Outage risk assessment team (ORAT) report to onsite safety review committee

Reactor shutdown, cooldown, and vessel disassembly

Refueling operations, fuel sipping, and off loaded fuel inspections

Daily/shiftly shutdown operations protection plan assessments

Shutdown postscram report to onsite safety review committee

Reactor recirculation pump trip logic modification installation and testing

Main steam line local leak rate testing

Transformer RSS1 offsite power line equipment inspection and upgrade

Division II to Division I protected division swap

Infrequently performed test or evolution briefings for:

- Divisional loss of offsite power/loss of coolant accident testing

- Concurrent control rod mechanism and blade changeout

- Reactor vessel pressure test and scram time testing

- Reactor startup, heatup, and power ascension

- Onsite safety review committee meeting to recommend startup

- Drywell 900 psi walkdown (after shutdown and during startup)

Documents reviewed by the inspectors are listed in the attachment.

The inspectors completed one inspection sample.

b.

Findings

Introduction: An NRC identified NCV of 10 CFR 50.65, Maintenance Rule,

Section (a)(4) was identified for the failure of the licensee to provide prescribed

compensatory measures for the highest shutdown risk condition during RFO-13.

Specifically, the preoutage risk assessment recommended that two WOs be in place for

maintenance electricians to provide power to one spent fuel pool cooling pump in the

event of problems with the running pump during periods of safety-related electrical bus

maintenance. The inspectors found that the WOs were not in place before entering

shutdown risk condition Orange on April 26, 2006, during the Division II ESF bus testing,

and on May 3, 2006, during the Division I ESF bus outage.

Description: The inspectors observed the onsite safety review committee meeting to

discuss and approve the ORAT report for RFO-13. The report noted two Orange

shutdown risk conditions for spent fuel pool cooling (SFC). Only one SFC pump would

be available after the beginning of core offload: (1) during the Division II ESF bus

testing with the SFC-P1B breaker racked out, and (2) during the Division I ESF bus

outage when SFC-P1A was without power. As a result of the ORAT review of

Enclosure

-19-

Procedure AOP-0051, Loss of Decay Heat Removal, Revision 17, they recommended

that the planned maintenance optimization group develop WOs for maintenance

electricians to provide alternate power from the station blackout diesel generator to the

deenergized SFC pump in the event of a failure of the running pump.

In addition, Procedure OSP-0037, Shutdown Operations Protection Plan, Revision 16,

Section 4.7, Fuel Pool Cooling, required that: (1) if work was required on SFC during

the outage, then it should be done as early as possible in the outage and not after fuel

offload (when heat load is the highest); and (2) if work was required after fuel offload,

then a contingency plan shall be in place prior to removing the system from service.

The inspectors determined that this requirement applied to deenergizing an SFC pump

for electrical bus maintenance.

On May 3, 2006, during the Division I ESF bus outage, the inspectors asked the

operations shift manager if the required WO was available to provide alternate power to

SFC-P1A in the event that the running SFC-P1B failed. He stated that he assumed that

the WO was written and that he would check. The inspectors then requested a copy of

the WO and a senior work planner reported that the WO was not available since it was

not yet approved for use in the electronic work planning program. Following discussions

with operators in the work management center, the licensee immediately took actions to

ensure that both WOs were processed and made ready for use.

The inspectors reviewed AOP-0051, Attachment 1, Spent Fuel Pool Curves, and

determined that the approximate time to boil for the spent fuel pool at that time with

offload fuel in the pool was approximately 8 hours9.259259e-5 days <br />0.00222 hours <br />1.322751e-5 weeks <br />3.044e-6 months <br />. Based on that data and the time

needed to generate the WOs, the inspectors determined that there was adequate time

for the licensee to connect an alternate power supply to the SFC pumps before the

spent fuel pool water started to boil if there was a failure of the running pump.

Analysis: The performance deficiency associated with this finding involved the failure to

establish prescribed compensatory measures for the highest outage risk condition

during RFO-13 as required by the shutdown operations protection plan. The finding was

more than minor because the licensee failed to implement prescribed compensatory

measures and failed to effectively manage those measures. The finding affected the

mitigating system cornerstone because of the increased risk of a sustained loss of SFC

during core offloading operations. The finding could not be evaluated using the

significance determination process; therefore, the finding was reviewed by regional

management and determined to be of very low safety significance. Factors that were

considered included: (1) electrical maintenance technicians had previously performed

the task of providing alternate power to an SFC pump, (2) the necessary equipment was

staged as part of the abnormal operating procedure for loss of decay heat removal, and

(3) the relatively long time to boil of the spent fuel storage pool at that time during the

refueling outage. The cause of the finding was related to the crosscutting aspect of

human performance because the licensees planned maintenance activities and the

predetermined increase in outage risk was not effectively managed by prescribed

compensatory measures.

Enclosure

-20-

Enforcement: 10 CFR 50.65(a)(4) requires, in part, that before performing maintenance

activities, the licensee shall assess and manage the increase in risk that may result from

the proposed maintenance activities. Contrary to this, the licensee failed to properly

manage the highest outage risk condition of RFO-13. On April 26, 2006, the plant

entered an Orange outage risk condition for SFC during core offload, when SFC-P1B

was deenergized for Division II ESF bus testing. On May 3, 2006, the plant entered an

Orange outage risk condition for SFC during core offload, when SFC-P1A was

deenergized for a Division I ESF bus outage. WOs were not written and ready for use

to have electricians provide alternate power to an SFC pump in the event the running

pump failed. The root cause involved the failure of the licensee to ensure that the WO

was in place before the plant entered the Orange shutdown risk condition. Corrective

action was taken to process the WOs for immediate use. Because the finding was of

very low safety significance and was entered into the licensees CAP as CR-RBS-2006-

01937, this violation is being treated as an NCV consistent with Section VI.A of the

Enforcement Policy: NCV 05000458/2006003-02, "Failure to adequately manage an

increase in plant risk."

1R22

Surveillance Testing

a.

Inspection Scope

The inspectors reviewed the USAR, procedure requirements, and TS to ensure that the

six surveillance activities listed below demonstrated that the SSCs tested were capable

of performing their intended safety functions. The inspectors either witnessed or

reviewed test data to verify that the following significant surveillance test attributes were

adequate: (1) preconditioning; (2) evaluation of testing impact on the plant;

(3) acceptance criteria; (4) test equipment; (5) procedures; (6) jumper/lifted lead

controls; (7) test data; (8) testing frequency and method demonstrated TS operability;

(9) test equipment removal; (10) restoration of plant systems; (11) fulfillment of ASME

Code requirements; (12) updating of performance indicator (PI) data; (13) engineering

evaluations, root causes, and bases for returning tested SSCs not meeting the test

acceptance criteria were correct; (14) reference setting data; and (15) annunciator and

alarm setpoints. The inspectors also verified that the licensee identified and

implemented any needed corrective actions associated with the surveillance testing.

STP-208-3601, "A Main Steam Line MSIVs and Outboard Drain Valve Leak

Rate Test and Inboard MSIV Inleakage Test," Revision 6, performed on May 2,

2006

STP-305-1606, [Division I Battery] ENB-BAT1A Service Discharge Test,

Revision 17, performed on May 6, 2006

STP-050-3601, Shutdown Margin Demonstration, Revision 27, performed on

May 12, 2006

STP-000-0102, Power Distribution Alignment Check, Revision 5, performed on

May 14 and 15, 2006

Enclosure

-21-

STP-508-4543, Turbine First Stage Pressure Channel Functional Test,

Revision 7, performed on June 4, 2006

Reactor coolant sample using Procedures COP-0001, Sampling via Various

Balance-Of-Plant Systems, Attachment 8, Reactor Sample Panel Routine

Sample Points, Revision 14, and COP-0305, Operation of the Countroom

Analysis Systems, Revision 2, performed on June 15, 2006

Documents reviewed by the inspectors are listed in the attachment.

The inspectors completed six inspection samples.

h.

Findings

Introduction: The inspectors identified an NCV of TS 5.4.1.a for the failure of the

licensee to provide an adequate surveillance test procedure to perform TS Surveillance

Requirement (SR) 3.8.1.1. Specifically, STP-000-0102, Power Distribution Alignment

Check, Revision 4, did not include steps to verify the required offsite power circuit

breaker alignment and indicated power availability for the Division III 4.16 kV ESF bus

as required in Modes 1, 2, and 3.

Description: As discussed in Section 1R15 of this report, operators failed to properly

rack in Breaker NNS-ACB23 on April 29, 2006. This condition was discovered on

May 22, when the breaker failed to close. During this period, on May 14, 2006, the

Division I EDG was removed from service to replace a leaking section of jacket cooling

water vent tubing. With the Division I EDG removed from service, TS Required

Action 3.8.1.a.1 required that operators perform TS SR 3.8.1.1 within one hour and

once every 8 hours9.259259e-5 days <br />0.00222 hours <br />1.322751e-5 weeks <br />3.044e-6 months <br /> until the EDG was operable. TS SR 3.8.1.1 required operators to

verify the correct breaker alignment and indicated power for each required offsite power

circuit. Operators utilized Procedure STP-000-0102, Power Distribution Alignment

Check, Revision 4, to satisfy the requirements of TS SR 3.8.1.1; however, the

inspectors identified that the procedure did not have steps to verify the correct breaker

alignment and indicated power availability to the Division III 4.16 kV ESF bus. As a

result, the operators did not identify that Breaker NNS-ACB23 was not racked in.

During the period that the Division I EDG was removed from service, the plant was

actually in TS Condition 3.8.1.d. TS Condition 3.8.1.d states that with One required

offsite circuit inoperable AND one required [E]DG inoperable, restore the EDG or the

offsite power supply to an operable status in 12 hours1.388889e-4 days <br />0.00333 hours <br />1.984127e-5 weeks <br />4.566e-6 months <br /> or place the plant in Mode 3 within

the next 12 hours1.388889e-4 days <br />0.00333 hours <br />1.984127e-5 weeks <br />4.566e-6 months <br />. The Division I EDG was inoperable for 15 hours1.736111e-4 days <br />0.00417 hours <br />2.480159e-5 weeks <br />5.7075e-6 months <br /> and 15 minutes.

Procedure STP-000-0102, Section 1.1, states, in part, that its purpose is to verify the

correct breaker alignment and indicated power availability for each required offsite

power circuit in accordance with TS SR 3.8.1.1 in Modes 1, 2, and 3. TS 3.8.1 bases

defines an offsite power circuit as follows: Each offsite circuit consists of incoming

breakers and disconnects to the respective preferred station service Transformers 1C

and 1D [RSS1 and RSS2], the 1C and 1D preferred station service transformers, and

the respective circuit path including feeder breakers to the three 4.16 kV ESF buses.

Enclosure

-22-

NNS-ACB23 is one of the circuit breakers between preferred station service

Transformer RTX-XSR1C and the Division III 4.16 kV ESF bus.

Analysis: The performance deficiency associated with this finding involved the

licensees failure to provide operators with an adequate STP to meet the requirements

of TS SR 3.8.1.1 to verify correct breaker alignment and indicated power availability to

the Division III ESF bus for each required offsite circuit. A review of previous revisions

of STP-000-0102 showed that the procedure has never verified the required offsite

power circuits for the Division III 4.16 kV ESF bus in Modes 1, 2, and 3. Although this

performance deficiency caused the failure to verify the offsite power circuit for an

extended period of time, the risk impact was limited to the 10 days from May 12-22,

2006. Therefore, the risk characterization of this finding is the same as that described in

Section 1R15 of this inspection report. The cause of the finding was related to the

crosscutting aspect of human performance because the licensee did not provide the

operators with an adequate STP to complete the TS SR to verify the required offsite

power circuits breaker alignment to all three 4.16 kV ESF buses. Additionally, the

cause of the finding was related to the crosscutting aspect of problem identification and

resolution in that on two occasions, June 18, 2005, and May 22, 2006, operators

entered TS Condition 3.8.1.a for one inoperable offsite power circuit to the Division III

4.16 kV ESF bus and performed STP-000-0102 to meet the Required Action to perform

SR 3.8.1.1, but did not recognize that STP-000-0102 did not verify the other offsite

power circuit breaker alignment to the Division III 4.16 kV ESF bus.

Enforcement: TS 5.4.1.a requires that written procedures be established, implemented,

and maintained covering the activities specified in Appendix A, "Typical Procedures for

Pressurized Water Reactors and Boiling Water Reactors," of Regulatory Guide 1.33,

"Quality Assurance Program Requirements (Operation)," dated February 1978.

Regulatory Guide 1.33, Appendix A, Section 8.a, requires procedures for all TS SRs.

Procedure STP-000-0102 states that it verified the correct breaker alignment and power

availability for each required offsite circuit in accordance with TS SR 3.8.1.1 in Modes 1,

2, and 3. Contrary to this, Procedure STP-000-0102, Revision 4, did not require

verification of the correct breaker alignment for the offsite power circuits to the

Division III 4.16 kV ESF bus in Modes 1, 2, and 3. The root cause involved the incorrect

interpretation of the Division III 4.16 kV bus SRs as they apply to the unique River Bend

Station ESF electrical distribution system. The corrective actions to restore compliance

included as an interim measure entering in the control room logs the breaker alignment

for and the bus voltage available to the Division III 4.16 kV ESF bus, until STP-000-0102

could be revised. Because the finding was of very low safety significance and has been

entered into the licensees CAP as CR-RBS-2006-02675 and -02402, this violation is

being treated as an NCV consistent with Section VI.A of the Enforcement Policy: NCV 05000458/2006003-03, Inadequate procedure to verify required offsite power breaker

alignment.

Enclosure

-23-

1R23

Temporary Plant Modifications

a.

Inspection Scope

The inspectors reviewed the USAR, plant drawings, procedure requirements, and TS to

ensure that Temporary Alteration 2006-0011, Off Gas Pretreatment Radiation Monitor

Sample Chamber Drain Line Modification, was properly implemented. The inspectors:

(1) verified that the modification did not have an affect on system operability/availability;

(2) verified that the installation was consistent with modification documents; (3) ensured

that the postinstallation test results were satisfactory and that the impact of the

temporary modification on the operation of the pretreatment radiation monitor were

supported by the test; (4) verified that the modification was identified on control room

drawings and that appropriate identification tags were placed on the affected drawings;

and (5) verified that appropriate safety evaluations were completed. The inspectors

verified that the licensee identified and implemented any needed corrective actions

associated with temporary modifications.

The inspectors completed one inspection sample.

b.

Findings

No findings of significance were identified.

Cornerstone: Emergency Preparedness

1EP6 Drill Evaluation

a.

Inspection Scope

On June 20, 2006, the inspectors observed the full scope exercise dress rehearsal,

which was used to contribute to Drill/Exercise Performance and Emergency Response

Organization Drill Performance PI. The inspectors: (1) observed the training evolution

to identify any weaknesses and deficiencies in classification, notification, and protective

action requirements development activities; (2) compared the identified weaknesses and

deficiencies against licensee identified findings to determine whether the licensee was

properly identifying failures; and (3) determined whether licensee performance was in

accordance with the guidance of the NEI 99-02, "Voluntary Submission of Performance

Indicator Data," Revision 2, acceptance criteria. The scenario used was RDRL-EP-

0602, Tornado/Loss of Offsite Power/Main Steam Line Break, dated June 16, 2006.

Emergency [plan] implementing procedures reviewed by the inspectors included:

EIP-2-001, Classification of Emergencies, Revision 13

EIP-2-006, Notifications, Revision 32

EIP-2-007, Protective Action Guidelines Recommendations, Revision 21

The inspectors completed one inspection sample.

Enclosure

-24-

b.

Findings

No findings of significance were identified.

2.

RADIATION SAFETY

Cornerstone: Occupational Radiation Safety

2OS1 Access Control to Radiologically Significant Areas

a.

Inspection Scope

This area was inspected to assess the licensees performance in implementing physical

and administrative controls for airborne radioactivity areas, radiation areas, high

radiation areas, and worker adherence to these controls. The inspector used the

requirements in 10 CFR Part 20, TS, and the licensees procedures required by TS as

criteria for determining compliance. During the inspection, the inspector interviewed the

radiation protection manager, radiation protection supervisors, and radiation workers.

The inspector performed independent radiation dose rate measurements and reviewed

the following items:

PI events and associated documentation packages reported by the licensee in

the occupational radiation safety cornerstone

Controls (surveys, posting, and barricades) of three radiation, high radiation, or

airborne radioactivity areas

Radiation work permits, procedures, engineering controls, and air sampler

locations

Conformation of electronic personal dosimeter alarm setpoints with survey

indications and plant policy; workers knowledge of required actions when their

electronic personnel dosimeter noticeably malfunctions or alarms

Barrier integrity and performance of engineering controls in airborne radioactivity

areas

Adequacy of the licensees internal dose assessment for any actual internal

exposure greater than 50 millirem committed effective dose equivalent

Physical and programmatic controls for highly activated or contaminated

materials (nonfuel) stored within spent fuel and other storage pools.

Self-assessments, audits, licensee event reports (LER), and special reports

related to the access control program since the last inspection

Corrective action documents related to access controls

Enclosure

-25-

Licensee actions in cases of repetitive deficiencies or significant individual

deficiencies

Radiation work permit briefings and worker instructions

Adequacy of radiological controls, such as required surveys, radiation protection

job coverage, and contamination controls during job performance

Dosimetry placement in high radiation work areas with significant dose rate

gradients

Changes in licensee procedural controls of high dose rate - high radiation areas

and very high radiation areas

Controls for special areas that have the potential to become very high radiation

areas during certain plant operations

Posting and locking of entrances to all accessible high dose rate - high radiation

areas and very high radiation areas

Radiation worker and radiation protection technician performance with respect to

radiation protection work requirements

The inspector completed 21 of the required 21 samples.

b.

Findings

1.

Unguarded High Radiation Area Boundary

Introduction: The inspector reviewed a self-revealing NCV of TS 5.7.1, resulting from

the licensees failure to control access to a high radiation area. The finding had very low

safety significance.

Description: On April 6, 2006, the licensee transferred reverse osmosis system filters

from one elevation of the radwaste building to another. Because dose rates on the filter

barrels were as high as 600 millirem per hour, the licensee assigned personnel to guard

the elevator entrances to prevent workers from entering high radiation areas. On this

occasion, the guards were not using radios, as was a common practice. Because of the

lack of good communication, a guard prematurely left his post in front of the 123-foot

elevation elevator door. Coincidently, two workers attempted to board the elevator on

the 123-foot elevation after the guard had left. The elevator carrying the barrels of

radioactive filters stopped at the 123-foot elevation, the doors opened, and the

electronic dosimeters of the workers alarmed because of the high dose rates. The

guard returned and evacuated the workers before they accrued additional radiation

dose. The highest dose rate recorded by an electronic alarming dosimeter was 164

millirem per hour. Planned corrective action was still being evaluated by the licensee at

the conclusion of the inspection.

Enclosure

-26-

Analysis: The failure to control access to a high radiation area was a performance

deficiency. The significance of the finding was greater than minor because it was

associated with the occupational radiation safety attribute of exposure control and

affected the cornerstone objective, in that not controlling access to a high radiation area

could increase personal exposure. Using the Occupational Radiation Safety

Significance Determination Process, the inspector determined that the finding was of

very low safety significance because it did not involve: (1) an as low as is reasonably

achievable (ALARA) finding, (2) an overexposure, (3) a substantial potential for

overexposure, or (4) an impaired ability to assess dose. Additionally, this finding had

crosscutting aspects associated with human performance in that the failure of the

individual to guard the elevator door directly contributed to the violation.

Enforcement: TS 5.7.1 requires each high radiation area, as defined in 10 CFR Part 20,

in which the intensity of radiation is greater than 100 millirems per hour but less than

1000 millirems per hour, be barricaded and conspicuously posted as a high radiation

area and entrance thereto shall be controlled by requiring issuance of a radiation work

permit. The licensee violated TS 5.7.1 when it failed to barricade and conspicuously

post the elevator housing the radioactive filter barrels or maintain a guard to ensure

workers did not enter a high radiation area. Because this failure to control a high

radiation area was of very low safety significance and has been entered into the

licensees CAP as CR-RBS-2006-01294, this violation is being treated as an NCV,

consistent with Section VI.A of the NRC Enforcement Policy:

NCV 05000458/2006003-04, Failure to control access to a high radiation area.

2.

Unanalyzed Airborne Radioactivity Survey

Introduction: The inspector identified an NCV of 10 CFR 20.1501(a) because the

licensee failed to survey airborne radioactivity. The finding had very low significance.

Description: On May 2, 2006, during the removal of local power range monitors, the

licensee started collecting an air sample of the work area. The air sample spanned two

shifts. A health physics technician on the second shift discarded the sample because

the first shift had not documented a start time. Therefore, the sample was never

analyzed. However, all workers successfully passed through the portal monitors at the

exit of the controlled access area without alarm, confirming that no worker experienced

an uptake of radioactive material. Planned corrective action is still being evaluated.

Analysis: The failure to survey airborne radioactivity was a performance deficiency.

This finding was greater than minor because it was associated with the occupational

radiation safety program attribute of exposure control and affected the cornerstone

objective in that the lack of knowledge of radiological conditions could increase

personnel dose. Using the Occupational Radiation Safety Significance Determination

Process, the inspector determined that the finding was of very low safety significance

because it did not involve: (1) an ALARA finding, (2) an overexposure, (3) a substantial

potential for overexposure, or (4) an impaired ability to assess dose. Additionally, this

finding had crosscutting aspects associated with human performance in that the failure

to maintain the sample for analysis directly contributed to the violation.

Enclosure

-27-

Enforcement: 10 CFR 20.1501(a) requires that each licensee make or cause to be

made surveys that may be necessary for the licensee to comply with the regulations in

10 CFR Part 20 and that are reasonable under the circumstances to evaluate the extent

of radiation levels, concentrations or quantities of radioactive materials, and the potential

radiological hazards that could be present. Pursuant to 10 CFR 20.1003, a survey

means an evaluation of the radiological conditions and potential hazards incident to the

production, use, transfer, release, disposal, or presence of radioactive material or other

sources of radiation. In part, 10 CFR 20.1201(a) states that the licensee shall control

the occupational dose to individual adults. The licensee violated 10 CFR 20.1501(a)

when it failed to perform an evaluation of airborne radioactivity to ensure compliance

with 10 CFR 20.1201(a). Because this failure to perform a radiological survey was of

very low safety significance and has been entered into the licensees CAP as

CR-RBS-2006-01994, this violation is being treated as an NCV, consistent with

Section VI.A of the NRC Enforcement Policy: NCV 05000458/2006003-05, Failure to

perform airborne radiation survey.

2OS2 ALARA Planning and Controls

a.

Inspection Scope

The inspector assessed licensee performance with respect to maintaining individual and

collective radiation exposures ALARA. The inspector used the requirements in 10 CFR Part 20 and the licensees procedures required by TS as criteria for determining

compliance. The inspector interviewed licensee personnel and reviewed:

Current 3-year rolling average collective exposure

Three outage or on-line maintenance work activities scheduled during the

inspection period and associated work activity exposure estimates which were

likely to result in the highest personnel collective exposures

ALARA work activity evaluations, exposure estimates, and exposure mitigation

requirements

Intended versus actual work activity doses and the reasons for any

inconsistencies

Shielding requests and dose/benefit analyses

Dose rate reduction activities in work planning

Use of engineering controls to achieve dose reductions and dose reduction

benefits afforded by shielding

Workers use of the low dose waiting areas

First-line job supervisors contribution to ensuring work activities are conducted

in a dose efficient manner

Enclosure

-28-

Radiation worker and radiation protection technician performance during work

activities in radiation areas, airborne radioactivity areas, or high radiation areas

The inspector completed 6 of the required 15 samples and 4 of the optional samples.

b.

Findings

No findings of significance were identified.

4.

OTHER ACTIVITIES

4OA1 Performance Indicator Verification

a.

Inspection Scope

1.

Barrier Integrity Cornerstone

The inspectors sampled licensee submittals for the two PIs listed below for the period

October 1, 2004, through March 31, 2006. The definitions and guidance of NEI 99-02,

Regulatory Assessment Indicator Guideline, Revision 4, were used to verify the

licensees basis for reporting each data element in order to verify the accuracy of PI

data reported during the assessment period. The inspectors: (1) reviewed reactor

coolant system (RCS) chemistry sample analyses for dose equivalent Iodine-131 and

compared the results to the TS limit; (2) observed a chemistry technician obtain and

analyze an RCS sample; (3) reviewed operating logs and surveillance results for

measurements of RCS identified leakage; and (4) observed a surveillance test that

determined RCS identified leakage.

C

RCS Specific Activity

C

RCS Leakage

The inspectors completed two inspection samples.

2.

Occupational Radiation Safety Cornerstone

The review included corrective action documentation that identified occurrences in

locked high radiation areas (as defined in the licensees TS), very high radiation areas

(as defined in 10 CFR 20.1003), and unplanned personnel exposures (as defined in

NEI 99-02), specifically CR-RBS-2006-01910. Additional records reviewed included

ALARA records and whole-body counts of selected individual exposures. The inspector

interviewed licensee personnel that were accountable for collecting and evaluating the

PI data. In addition, the inspector toured plant areas to verify that high radiation, locked

high radiation, and very high radiation areas were properly controlled. PI definitions and

guidance contained in NEI 99-02, "Regulatory Assessment Indicator Guideline,"

Revision 3, were used to verify the basis in reporting for each data element.

Enclosure

-29-

Occupational Exposure Control Effectiveness

The inspector completed the one required sample in this cornerstone.

3.

Public Radiation Safety Cornerstone

The inspector reviewed licensee documents from June 1, 2005, through March 31,

2006. Licensee records reviewed included corrective action documentation that

identified occurrences for liquid or gaseous effluent releases that exceeded PI

thresholds and those reported to the NRC. The inspector interviewed licensee

personnel that were accountable for collecting and evaluating the PI data. PI definitions

and guidance contained in NEI 99-02, "Regulatory Assessment Indicator Guideline,"

Revision 3, were used to verify the basis in reporting for each data element.

Radiological Effluent Technical Specification/Offsite Dose Calculation Manual

Radiological Effluent Occurrences

The inspector completed the one required sample in this cornerstone.

f.

Findings

No findings of significance were identified.

4OA2 Identification and Resolution of Problems

1.

Semiannual Trend Review

g.

Inspection Scope

The inspectors completed a semiannual trend review of repetitive or closely related

issues related to identify trends that might indicate the existence of more safety

significant issues. The inspectors review consisted of the 6-month period from

January 1 to June 30, 2006, of CAP items associated with the three EDG starting air

systems documented in 42 CRs. When warranted, some of the samples expanded

beyond those dates to fully assess the issue. The inspectors compared and contrasted

their results with the results contained in adverse trend CRs for problems related to the

starting air compressors and air dryers. Corrective actions associated with a sample of

the issues identified were reviewed for adequacy. The CRs reviewed by the inspectors

are listed in the attachment.

The inspectors completed one inspection sample.

b. Findings and Observations

There were no findings of significance identified associated with the CRs reviewed.

The inspectors noted that the licensee had identified a long-standing issue related to the

performance of the EDG starting air systems air compressors. Since January 1, 2006,

Enclosure

-30-

there were 18 CRs written for high metal wear products in monthly air compressor oil

samples. Each of these CRs was closed to CR-RBS-2004-02165. An additional

28 CRs written since August 2, 2004, for high metal wear product concentrations and

high moisture content in monthly compressor oil samples were closed to CR-RBS-2004-

02165. In addition, operators wrote adverse trend CR-RBS-2006-02407 to detail

compressor problems, including excessive run times. The inspectors determined that

the licensee is taking appropriate actions to understand the problem with the EDG

starting air compressors, including sending the system engineer to observe the vendors

teardown and refurbishment of two of the starting air compressors.

Another four CRs have been written since January 1, 2006, describing problems with

starting air system dryers and dryer prefilters. Following a June 29, 2006, meeting held

to discuss overall EDG starting air system maintenance problems, the licensee wrote

CR-RBS-2006-02799, to look into the relationship between the prefilter and dryer

problems. The inspectors noted that this meeting was the first discussion of the overall

condition of the EDG starting air systems and to evaluate the interrelationship between

compressor, dryer, and prefilter problems.

2.

Occupational Radiation Safety

a.

Inspection Scope

The inspector evaluated the effectiveness of the licensees problem identification and

resolution process with respect to the following inspection areas:

Access Control to Radiologically Significant Areas (Section 2OS1)

ALARA Planning and Controls (Section 2OS2)

b. Findings and Observations

No findings of significance were identified.

3.

Inservice Inspection Activities

a.

Inspection Scope

The inspector reviewed selected inservice inspection related CRs issued during the

current and past refueling outages. The review served to verify that the licensees CAP

was being correctly utilized to identify conditions adverse to quality and that those

conditions were being adequately evaluated, corrected, and trended.

b.

Findings

No findings of significance were identified.

Enclosure

-31-

4OA3 Event Followup

1.

(Closed) LER 50-458/2004-003-01, Unplanned Automatic Start of Standby Diesel

Generator Due to Loss of Division 1 Switchgear

On October 31, 2004, technicians caused an unexpected degraded voltage signal,

which resulted in a loss of the Division I 4.16 kV ESF bus during preparations for the

Division I loss of offsite power/loss of coolant accident test. The Division I EDG

automatically started and powered the ESF bus and all equipment operated as

expected. Initial inspection of this event was documented in NRC integrated inspection

Report 05000458/2004005. During this inspection period, the inspectors reviewed the

LER, the root cause analysis, and corrective actions documented in

CR-RBS-2004-03518. No additional findings of significance were identified. This LER

is closed.

2.

(Closed) LER 50-458/2004-004-01, Unplanned Automatic Start of Standby Diesel

Generator Due to Loss of Division 2 Switchgear

On November 1, 2004, technicians inadvertently caused a trip of Transformer RSS2

preferred station service Transformer RTX-XSR1F while troubleshooting a transformer

sudden pressure relay trip circuit. As a result, power was also lost to preferred station

Transformer RTX-XSR1D and the Division II 4.16 kV ESF bus. The running shutdown

cooling, alternate decay heat removal, and plant operating water cleanup systems lost

power until the Division II EDG started and restored power to the ESF bus. Shutdown

cooling was restored in less than one hour. Initial inspection of this event was

documented in NRC integrated inspection Report 05000458/2004005. During this

inspection period, the inspectors reviewed the LER, the root cause analysis, and

corrective actions documented in CR-RBS-2004-03546. No additional findings of

significance were identified. This LER is closed.

3.

(Closed) LER 50-458/2004-005-01, Unplanned Automatic Scram Due to Loss of

Non-Vital 120 Volt Instrument Bus

On December 10, 2004, an automatic scram occurred due to a loss of power to

nonsafety-related instrumentation Bus VBN-PNL01B1. A capacitor on the control board

for the nonsafety-related Inverter BYS-INV01B static switch failed, which caused a loss

of power to Bus VBN-PNL01B1, a subsequent downshift of the plant operating

recirculation pumps and a lockup of the main feedwater regulating valves. The result

was an automatic plant scram complicated by a loss of normal feedwater. Inspection of

this event was documented in NRC integrated inspection Report 05000458/2004005.

Additional inspection was documented in NRC supplemental inspection Report

05000458/2005012. During this inspection period, the inspectors reviewed the LER, the

root cause analysis, and corrective actions documented in CR-RBS-2004-04289. No

additional findings of significance were identified. This LER is closed.

Enclosure

-32-

4.

(Closed) LER 50-458 /2005-001-01, Unplanned Manual Scram Due to Indication of

Ground Fault in Main Generator

On January 15, 2005, while the plant was at 100 percent power, a main generator field

ground fault alarm was received. Control room operators tripped the turbine in

accordance with alarm response Procedure ARP-680-09. The licensee later determined

that one of the five rectifier banks in the generator excitation control system was the

source of the ground and removed it from service. In addition, the licensee tested the

relay that causes the main generator ground fault alarm and found it to be out of

calibration such that it alarmed before the ground current reached its setpoint. The

alarm response procedure requirement to trip the turbine was revised to allow validation

of the alarm before tripping the main turbine. Inspection of this event was documented

in NRC integrated inspection Report 05000458/2005002. Additional inspection was

documented in NRC supplemental inspection Report 05000458/2005012. During this

inspection period, the inspectors reviewed the LER, the root cause analysis, and

corrective actions documented in CR-RBS-2005-00140. No additional findings of

significance were identified. This LER is closed.

4OA5 Other Activities

Implementation of Temporary Instruction 2515/165 - Operational Readiness of Offsite

Power and Impact on Plant Risk

a.

Inspection Scope

The objective of Temporary Instruction 2515/165, "Operational Readiness of Offsite

Power and Impact on Plant Risk," was to gather information to support the assessment

of nuclear power plant operational readiness of offsite power systems and impact on

plant risk. During this inspection, the inspectors interviewed licensee personnel,

reviewed licensee procedures, and gathered information for further evaluation by the

Office of Nuclear Reactor Regulation.

b.

Findings

No findings of significance were identified.

4OA6 Meetings, Including Exit

Exit Meetings

On May 5, 2006, the inspector presented the occupational radiation safety inspection

results to Mr. D. Vinci, General Manager, Plant Operations, and other members of his

staff who acknowledged the findings. The inspector confirmed that proprietary

information was not provided or examined during the inspection.

On May 5, 2006, the inspector presented the results of this inspection of inservice

inspection activities to Mr. P. Russell, Manager, System Engineering, and other

Enclosure

-33-

members of licensee management. The inspector confirmed that proprietary

information was not provided or examined during the inspection.

On July 5, 2006, the resident inspectors presented the integrated baseline inspection

results to Mr. P. Hinnenkamp, Vice President - Operations, and other members of

licensee management. The inspectors confirmed that proprietary information was not

provided or examined during the inspection.

ATTACHMENT: SUPPLEMENTAL INFORMATION

Attachment

A-1

SUPPLEMENTAL INFORMATION

KEY POINTS OF CONTACT

Licensee Personnel

T. Baccus, Acting Supervisor, ALARA Planning

L. Ballard, Manager, Quality Programs

D. Burnett, Superintendent, Chemistry

C. Bush, Manager, Outage

J. Clark, Assistant Operations Manager - Training

T. Coleman, Manager, Planning and Scheduling/Outage

M. Davis, Manager, Radiation Protection

C. Forpahl, Manager, Corrective Action Program

T. Gates, Manager, Equipment Reliability

H. Goodman, Director, Engineering

K. Higginbotham, Assistant Operations Manager - Shift

P. Hinnenkamp, Vice President - Operations

B. Houston, Manager, Plant Maintenance

A. James, Superintendent, Plant Security

K. Jenks, Supervisor, Engineering Codes and Standards

N. Johnson, Manager, Engineering Programs & Components

R. King, Director, Nuclear Safety Assurance

J. Leavines, Manager, Emergency Planning

D. Lorfing, Manager, Licensing

J. Maher, Superintendent, Reactor Engineering

W. Mashburn, Manager, Design Engineering

J. Miller, Manager, Training and Development

P. Russell, Manager, System Engineering

C. Stafford, Manager, Operations

D. Vinci, General Manager - Plant Operations

LIST OF ITEMS OPENED, CLOSED, AND DISCUSSED

Opened and Closed

05000458/2006003-01

NCV

Failure to identify Division III ESF bus supply breaker not

racked in

05000458/2006003-02

NCV

Failure to adequately manage an increase in plant risk 05000458/2006003-03

NCV

Inadequate procedure to verify required offsite power

breaker alignment

05000458/2006003-04

NCV

Failure to control access to a high radiation area

05000458/2006003-05

NCV

Failure to perform airborne radiation survey

Attachment

A-2

Closed

50-458/2004-003-01

LER

Unplanned Automatic Start of Standby Diesel Generator

Due to Loss of Division 1 Switchgear

50-458/2004-004-01

LER

Unplanned Automatic Start of Standby Diesel Generator

Due to Loss of Division 2 Switchgear

50-458/2004-005-01

LER

Unplanned Automatic Scram Due to Loss of Non-Vital 120

Volt Instrument Bus

50-458 /2005-001-01

LER

Unplanned Manual Scram Due to Indication of Ground

Fault in Main Generator

LIST OF DOCUMENTS REVIEWED

The following documents were selected and reviewed by the inspectors to accomplish the

objectives and scope of the inspection and to support any findings:

Section 1R06: Inservice Inspection Activities

Procedures

CEP-NDE-0400, Ultrasonic Examination, Revision 0

CEP-NDE-0404, Manual Ultrasonic Examination of Ferritic Piping Welds (ASME XI),

Revision 1

CEP-NDE-0407, Straight Beam Ultrasonic Examination of Bolts and Studs (ASME XI),

Revision 1

CEP-NDE-0423, Manual Ultrasonic Examination of Austenitic Piping Welds (ASME XI),

Revision 1

CEP-NDE-0424, Manual Ultrasonic Examination of the Reactor Vessel Flange Ligament Areas

(ASME XI), Revision 1

CEP-NDE-0428, Manual Ultrasonic Throughwall Sizing in Piping Welds (ASME XI), Revision 1

CEP-NDE-0641, Liquid Penetrant Examination for ASME Section XI, Revision 1

CEP-NDE-0731, Magnetic Particle Examination (ASME Section XI), Revision 0

SPP-7010, Preparation of Weld Data Documents, Revision 9

Attachment

Miscellaneous Documents

7228.000-701-131A, Risk Informed Break Exclusion Region Evaluation for River Bend

Station, Revision 0

Liquid Penetrant Examinations

BOP-PT-06-024

BOP-PT-06-025

BOP-PT-06-026

BOP-PT-06-029

UT Calibration Reports

CAL -06-015

CAL -06-016

CAL-06-017

UT Pipe Weld Examinations

ISI-UT-06-003

ISI-UT-06-006

ISI-UT-06-009

ISI-UT-06-012

ISI-UT-06-004

ISI-UT-06-007

ISI-UT-06-010

ISI-UT-06-013

ISI-UT-06-005

ISI-UT-06-008

ISI-UT-06-011

ISI-UT-06-014

Condition Reports

CR-RBS-2005-00065

CR-RBS-2005-00067

CR-RBS-2005-00100

CR-RBS-2005-01379

Section 1R15: Operability Evaluations

Primary Containment Purge Exhaust Line Operability

CR-RBS-2006-00964, primary containment purge exhaust line leak rate test results showing

negative trend

ADM-0050, Primary Containment Leakage Rate Testing Program, Revision 8

SEP-APJ-001, Primary containment Leakage Rate Testing (Appendix J) Program,

Revision 0G

STP-403-7301, Containment Purge System Isolation Valve Leak Rate Test, Revisions 0, 1, 2,

and 3

RBS-ER-00-0589, Post RF-09 LLRT Testing Interval Determination, dated January 25, 2001

RBS TS Amendment 81, dated July 20, 1995

RBS TS Bases Revision 126, dated March 31, 206

Attachment

A-4

NNS-ACB23 Not Functional

Electrical Drawings

EE-001AC, Startup Electrical Distribution Chart, Revision 33

ESK-05NNS03, Elementary Diagram - 4.16 kV Switchgear Bus 1C Normal Supply ACB,

Revision 13

Corrective Action Documents

CR-RBS-2006-02402

CR-RBS-2006-0235

CR-RBS-2006-02337

CR-RBS-1998-00190

Procedures

OSP-0022, Operations General Administrative Guidelines, Revision 01

GOP-0001, Plant Startup, Revision 47, performed on May 12, 2006

STP-000-0102, Power Distribution Alignment Check, Revision 4, performed on May 9, 2006

STP-000-0102, Power Distribution Alignment Check, Revision 4, performed on May 22, 2006

Work Requests

WR 76625

WR 77441

WR77478

Miscellaneous Documents

Main Control Room Logs

TS LCO Records: 1-OPT-06-0187

1-TS-06-0694

RBS Tagout Record: 1-302-NNS-SWG1A-006-A

Section 1R20: Refueling and Other Outage Activities

Procedures

RSP-0217, Auxiliary Access Control Functions, Revision 27

GOP-0003, Scram Recovery, Revision 14A, post scram report, dated April 23, 2006

OSP-0031, Shutdown Operations Protection Plan, Revision 16

OSP-0041, Alternate Decay Heat Removal, Revision 8A

AOP-0051, Loss of Decay Heat Removal, Revision 18

OSP-0034, Control of Obstructions for Primary Containment/Fuel Building Operability,

Revision 3

Attachment

A-5

GOP-0001, Plant Startup, Revision 47, performed on May 12, 2006

Corrective Action Documents

CR-RBS-2006-00691

CR-RBS-2006-01937

Miscellaneous Documents

Control Room Logs

TS LCO Logs

Daily Refueling Outage Updates

ORAT Report

WO 50340401 and 81284

ER-RB-2005-0157-000, Install new relays on the output of EOC-RPT optical output cards

C71A-AT17 and C71A-AT18, dated May 16, 2006

WO 5034041's task outline to configure the station blackout diesel to supply power to spent fuel

pool cooling Pump SFC-P1A

WO 5034041, Configure the station blackout diesel to supply power to spent fuel pool cooling

Pump SFC-P1A, written May 3, 2006

Section 1R22: Surveillance Testing

Drawing EE-001AC, Startup Electrical Distribution Chart, Revision 33

TS Section 3.8.1 and Bases 3.8.1, Revision 0

USAR Section 8.2.1.2.1, General Design Criteria, Revision 16

NUREG-0989, Safety Evaluation Report Related to the Operation of River Bend Station,

dated May 1984

TS LCO Logs

1-TS-06-0694

I-TS-06-0685

1-TS-05-0386

Corrective Action Documents

CR-RBS-2006-02675

CR-RBS-2006-02402

CR-RBS-2005-02331

Attachment

A-6

Section 4OA2: Identification and Resolution of Problems

Semiannual Trend Review

CR-RBS-2004-02165

CR-RBS-2006-00159

CR-RBS-2006-00226

CR-RBS-2006-00279

CR-RBS-2006-00296

CR-RBS-2006-00434

CR-RBS-2006-00663

CR-RBS-2006-00798

CR-RBS-2006-00799

CR-RBS-2006-00928

CR-RBS-2006-00993

CR-RBS-2006-01131

CR-RBS-2006-01132

CR-RBS-2006-01205

CR-RBS-2006-01261

CR-RBS-2006-01270

CR-RBS-2006-01324

CR-RBS-2006-01333

CR-RBS-2006-01429

CR-RBS-2006-01464

CR-RBS-2006-01489

CR-RBS-2006-01490

CR-RBS-2006-02269

CR-RBS-2006-02348

CR-RBS-2006-02349

CR-RBS-2006-02356

CR-RBS-2006-02375

CR-RBS-2006-02406

CR-RBS-2006-02407

CR-RBS-2006-02469

CR-RBS-2006-02484

CR-RBS-2006-02540

CR-RBS-2006-02544

CR-RBS-2006-02550

CR-RBS-2006-02558

CR-RBS-2006-02559

CR-RBS-2006-02651

CR-RBS-2006-02661

CR-RBS-2006-02682

CR-RBS-2006-02683

CR-RBS-2006-02732

CR-RBS-2006-02733

CR-RBS-2006-02799

Section 2OS1: Access Controls to Radiologically Significant Areas

Corrective Action Documents

CR-RBS-2006-00090 CR-RBS- 2006-01294 CR-RBS-2006-01787 CR-RBS- 2006-01950

Radiation Work Permits

2006-1915

RFO-13, Remove and Replace LPRMs, Including Support Activities

2006-1921

RFO-13, Flow Control Valve Maintenance, Including Support Activities

2006-1929

RFO-13, Recirc Pump Work, Including Support Activities

Procedures

RP-103

Access Control, Revision 2

RP-106

Radiological Survey Documentation, Revision 1

RP-108

Radiation Protection Posting, Revision 2

RPP-0006

Performance of Radiological Surveys, Revision 19

Section 2OS2: ALARA Planning and Controls (71121.02)

Corrective Action Documents

CR-RBS-2006-01746

Procedures

ENS-RP-105 Radiation Work Permits, Revision 7

Attachment

A-7

LIST OF ACRONYMS

CDF

core damage frequency

ALARA

as low as is reasonably achievable

ASME

American Society of Mechanical Engineers

CAP

corrective action program

CFR

Code of Federal Regulations

CR-RBS

River Bend Station condition report

EDG

emergency diesel generator

LER

licensee event report

MC

inspection manual chapter

NCV

noncited violation

NDE

nondestructive examination

NEI

Nuclear Energy Institute

NRC

U.S. Nuclear Regulatory Commission

ORAT

outage risk assessment team

PI

performance indicators

RCS

reactor coolant system

RFO

refueling outage

SFC

spent fuel pool cooling system

SOP

system operating procedures

SR

surveillance requirement

SSC

structures, systems, or components

STP

surveillance test procedure

TS

Technical Specifications

USAR

Updated Safety Analysis Report

WO

work order

WR

work request