IR 05000263/2016008: Difference between revisions

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=Text=
=Text=
{{#Wiki_filter:UNITED STATES ril 26, 2016
{{#Wiki_filter:April 26, 2016


==SUBJECT:==
==SUBJECT:==
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Sincerely,
Sincerely,
/RA Dariusz Szwarc Acting for Robert C. Daley, Chief Engineering Branch 3 Division of Reactor Safety Docket No. 50-263 License No. DPR-22
/RA Dariusz Szwarc Acting for  
 
Robert C. Daley, Chief Engineering Branch 3 Division of Reactor Safety Docket No. 50-263 License No. DPR-22  


===Enclosure:===
===Enclosure:===
IR 05000263/2016008
IR 05000263/2016008  


REGION III==
REGION III==
Docket No: 50-263 License No: DPR-22 Report No: 05000263/2016008 Licensee: Northern States Power Company, Minnesota Facility: Monticello Nuclear Generating Plant Location: Monticello, MN Dates: February 29 thru March 24, 2016 Inspectors: Alan Dahbur, Senior Reactor Inspector (Lead)
Docket No:
Jorge J. Corujo-Sandín, Reactor Inspector Michael A. Jones, Reactor Inspector Approved by: Robert C. Daley, Chief Engineering Branch 3 Division of Reactor Safety Enclosure
50-263 License No:
DPR-22 Report No:
05000263/2016008 Licensee:
Northern States Power Company, Minnesota Facility:
Monticello Nuclear Generating Plant Location:
Monticello, MN Dates:
February 29 thru March 24, 2016 Inspectors:
Alan Dahbur, Senior Reactor Inspector (Lead)
Jorge J. Corujo-Sandín, Reactor Inspector Michael A. Jones, Reactor Inspector Approved by:
Robert C. Daley, Chief Engineering Branch 3 Division of Reactor Safety  


=SUMMARY=
=SUMMARY=
Inspection Report 05000263/2016008; 02/29/2016 - 03/24/2016; Monticello Nuclear Generating
Inspection Report 05000263/2016008; 02/29/2016 - 03/24/2016; Monticello Nuclear Generating  


Plant; Evaluations of Changes, Tests, and Experiments and Permanent Plant Modifications.
Plant; Evaluations of Changes, Tests, and Experiments and Permanent Plant Modifications.
Line 59: Line 70:


===Licensee-Identified Violations===
===Licensee-Identified Violations===
No violations were identified.
No violations were identified.


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==REACTOR SAFETY==
==REACTOR SAFETY==
Cornerstones: Initiating Events, Mitigating Systems, and Barrier Integrity
Cornerstones: Initiating Events, Mitigating Systems, and Barrier Integrity {{a|1R17}}
{{a|1R17}}
 
==1R17 Evaluations of Changes, Tests, and Experiments and Permanent Plant Modifications==
==1R17 Evaluations of Changes, Tests, and Experiments and Permanent Plant Modifications==
{{IP sample|IP=IP 71111.17T}}
{{IP sample|IP=IP 71111.17T}}
===.1 Evaluation of Changes, Tests, and Experiments===
===.1 Evaluation of Changes, Tests, and Experiments===
====a. Inspection Scope====
The inspectors reviewed 4 safety evaluations performed pursuant to Title 10, Code of Federal Regulations (CFR), Part 50, Section 59, to determine if the evaluations were adequate, and that prior U.S. Nuclear Regulatory Commission (NRC) approval was obtained as appropriate. The inspectors also reviewed 13 screenings where licensee personnel had determined that a 10 CFR 50.59 evaluation was not necessary. The inspectors reviewed these documents to determine if:


====a. Inspection Scope====
the changes, tests, and experiments performed were evaluated in accordance with 10 CFR 50.59 and that sufficient documentation existed to confirm that a license amendment was not required;  
The inspectors reviewed 4 safety evaluations performed pursuant to Title 10, Code of Federal Regulations (CFR), Part 50, Section 59, to determine if the evaluations were adequate, and that prior U.S. Nuclear Regulatory Commission (NRC) approval was obtained as appropriate. The inspectors also reviewed 13 screenings where licensee personnel had determined that a 10 CFR 50.59 evaluation was not necessary. The inspectors reviewed these documents to determine if:
 
the changes, tests, and experiments performed were evaluated in accordance with 10 CFR 50.59 and that sufficient documentation existed to confirm that a license amendment was not required; the safety issue requiring the change, tests or experiment was resolved; the licensee conclusions for evaluations of changes, tests, and experiments were correct and consistent with 10 CFR 50.59; and the design and licensing basis documentation was updated to reflect the change.
the safety issue requiring the change, tests or experiment was resolved;  
 
the licensee conclusions for evaluations of changes, tests, and experiments were correct and consistent with 10 CFR 50.59; and  
 
the design and licensing basis documentation was updated to reflect the change.


The inspectors used, in part, Nuclear Energy Institute Document 96-07, Guidelines for 10 CFR 50.59 Implementation, Revision 1, to determine acceptability of the completed evaluations, and screenings. The Nuclear Energy Institute document was endorsed by the NRC in Regulatory Guide 1.187, Guidance for Implementation of 10 CFR 50.59, Changes, Tests, and Experiments, dated November 2000. The inspectors also consulted Part 9900 of the NRC Inspection Manual, 10 CFR Guidance for 10 CFR 50.59, Changes, Tests, and Experiments.
The inspectors used, in part, Nuclear Energy Institute Document 96-07, Guidelines for 10 CFR 50.59 Implementation, Revision 1, to determine acceptability of the completed evaluations, and screenings. The Nuclear Energy Institute document was endorsed by the NRC in Regulatory Guide 1.187, Guidance for Implementation of 10 CFR 50.59, Changes, Tests, and Experiments, dated November 2000. The inspectors also consulted Part 9900 of the NRC Inspection Manual, 10 CFR Guidance for 10 CFR 50.59, Changes, Tests, and Experiments.
Line 80: Line 97:


====b. Findings====
====b. Findings====
(Open) Unresolved Item 05000263/2016008-01, Failure to provide acceptable Alternate Methods of Decay Heat Removal
(Open) Unresolved Item 05000263/2016008-01, Failure to provide acceptable Alternate Methods of Decay Heat Removal  


=====Introduction:=====
=====Introduction:=====
The inspectors identified an Unresolved Item associated with Technical Specification (TS) 3.4.8, Residual Heat Removal (RHR) Shutdown Cooling System -
The inspectors identified an Unresolved Item associated with Technical Specification (TS) 3.4.8, Residual Heat Removal (RHR) Shutdown Cooling System - Cold Shutdown. Specifically, the licensee failed to verify that the capability of the alternate methods of decay heat removal described in Operations Manual C.4-B.03.04.A, Loss of Normal Shutdown Cooling, were adequate to combat a loss of shutdown cooling resulting from the loss of one or two RHR subsystems while in MODE 4 with high decay heat load.
Cold Shutdown. Specifically, the licensee failed to verify that the capability of the alternate methods of decay heat removal described in Operations Manual C.4-B.03.04.A, Loss of Normal Shutdown Cooling, were adequate to combat a loss of shutdown cooling resulting from the loss of one or two RHR subsystems while in MODE 4 with high decay heat load.


=====Description:=====
=====Description:=====
Line 102: Line 118:


===.2 Permanent Plant Modifications===
===.2 Permanent Plant Modifications===
====a. Inspection Scope====
The inspectors reviewed 8 permanent plant modifications that had been installed in the plant during the last 3 years. This review included in-plant walkdowns portions of the high-pressure coolant injection steam drain line system, the Emergency Diesel Generator Fuel Oil Transfer System, including the Diesel Fuel Oil pump house, the new diesel fuel oil pumps installed in the day tank room, and portions of the fuel oil storage tank tornado missile protection modifications. The modifications were selected based upon risk significance, safety significance, and complexity. The inspectors reviewed the modifications selected to determine if:
the supporting design and licensing basis documentation was updated;
the changes were in accordance with the specified design requirements;
the procedures and training plans affected by the modification have been adequately updated;
the test documentation as required by the applicable test programs has been updated; and


====a. Inspection Scope====
post-modification testing adequately verified system operability and/or functionality.
The inspectors reviewed 8 permanent plant modifications that had been installed in the plant during the last 3 years. This review included in-plant walkdowns portions of the high-pressure coolant injection steam drain line system, the Emergency Diesel Generator Fuel Oil Transfer System, including the Diesel Fuel Oil pump house, the new diesel fuel oil pumps installed in the day tank room, and portions of the fuel oil storage tank tornado missile protection modifications. The modifications were selected based upon risk significance, safety significance, and complexity. The inspectors reviewed the modifications selected to determine if:
the supporting design and licensing basis documentation was updated; the changes were in accordance with the specified design requirements; the procedures and training plans affected by the modification have been adequately updated; the test documentation as required by the applicable test programs has been updated; and post-modification testing adequately verified system operability and/or functionality.


The inspectors also used applicable industry standards to evaluate acceptability of the modifications. The list of modifications and other documents reviewed by the inspectors is included as an Attachment to this report.
The inspectors also used applicable industry standards to evaluate acceptability of the modifications. The list of modifications and other documents reviewed by the inspectors is included as an Attachment to this report.
Line 113: Line 137:
==OTHER ACTIVITIES==
==OTHER ACTIVITIES==
{{a|4OA2}}
{{a|4OA2}}
==4OA2 Problem Identification and Resolution==
==4OA2 Problem Identification and Resolution==
===.1 Routine Review of Condition Reports===
===.1 Routine Review of Condition Reports===
====a. Inspection Scope====
====a. Inspection Scope====
The inspectors reviewed several corrective action process documents that identified or were related to Title 10 of the Code of Federal Regulations, Part 50.59 evaluations and permanent plant modifications. The inspectors reviewed these documents to evaluate the effectiveness of corrective actions related to permanent plant modifications and evaluations of changes, tests, and experiments. In addition, corrective action documents written on issues identified during the inspection were reviewed to verify adequate problem identification and incorporation of the problems into the corrective action system. The specific corrective action documents that were sampled and reviewed by the inspectors are listed in the attachment to this report.
The inspectors reviewed several corrective action process documents that identified or were related to Title 10 of the Code of Federal Regulations, Part 50.59 evaluations and permanent plant modifications. The inspectors reviewed these documents to evaluate the effectiveness of corrective actions related to permanent plant modifications and evaluations of changes, tests, and experiments. In addition, corrective action documents written on issues identified during the inspection were reviewed to verify adequate problem identification and incorporation of the problems into the corrective action system. The specific corrective action documents that were sampled and reviewed by the inspectors are listed in the attachment to this report.
Line 122: Line 145:
====b. Findings====
====b. Findings====
No findings were identified.
No findings were identified.
{{a|4OA6}}


{{a|4OA6}}
==4OA6 Management Meetings==
==4OA6 Management Meetings==
 
===.1===
===.1 Exit Meeting Summary===
===Exit Meeting Summary===
 
On March 24, 2016, the inspectors presented the inspection results to Mr. M. Lingenfelter, and other members of the licensee staff. The licensee personnel acknowledged the inspection results presented and did not identify any proprietary content. The inspectors confirmed that all proprietary material provided to the inspection team was identified and will be dispositioned in accordance with applicable processes.
On March 24, 2016, the inspectors presented the inspection results to Mr. M. Lingenfelter, and other members of the licensee staff. The licensee personnel acknowledged the inspection results presented and did not identify any proprietary content. The inspectors confirmed that all proprietary material provided to the inspection team was identified and will be dispositioned in accordance with applicable processes.


Line 135: Line 157:


==KEY POINTS OF CONTACT==
==KEY POINTS OF CONTACT==
 
Licensee  
Licensee
: [[contact::M. Lingenfelter]], Director of Engineering  
: [[contact::M. Lingenfelter]], Director of Engineering
: [[contact::A. Gonnering]], Design Engineering  
: [[contact::A. Gonnering]], Design Engineering
: [[contact::M. Kelly]], Performance Assurance Manager  
: [[contact::M. Kelly]], Performance Assurance Manager
: [[contact::J. Gausman]], Engineering  
: [[contact::J. Gausman]], Engineering
: [[contact::A. Ward]], Regulatory Affairs Manager  
: [[contact::A. Ward]], Regulatory Affairs Manager
: [[contact::T. Hurrle]], Design Engineering Manager  
: [[contact::T. Hurrle]], Design Engineering Manager
: [[contact::B. Halvorson]], Engineering  
: [[contact::B. Halvorson]], Engineering
: [[contact::A. Kouba]], Regulatory Affairs  
: [[contact::A. Kouba]], Regulatory Affairs
: [[contact::D. Alstad]], Design Engineer  
: [[contact::D. Alstad]], Design Engineer
: [[contact::E. Watzel]], Electrical Design Engineering Supervisor
: [[contact::E. Watzel]], Electrical Design Engineering Supervisor
U.S. Nuclear Regulatory Commission
U.S. Nuclear Regulatory Commission  
: [[contact::P. Zurawski]], Senior Resident Inspector
: [[contact::P. Zurawski]], Senior Resident Inspector  
: [[contact::P. LaFlamme]], Acting Senior Resident Inspector
: [[contact::P. LaFlamme]], Acting Senior Resident Inspector  
: [[contact::D. Krause]], Resident Inspector
: [[contact::D. Krause]], Resident Inspector  


==LIST OF ITEMS==
==LIST OF ITEMS==
===OPENED, CLOSED AND DISCUSSED===
===OPENED, CLOSED AND DISCUSSED===
===Opened===
===Opened===
: 05000263/2016008-01 URI Failure to provide acceptable Alternate Methods of Decay Heat Removal (Section 1R17.1b)
Closed and


Failure to provide acceptable Alternate Methods of Decay Heat
: 05000263/2016008-01 URI Removal (Section 1R17.1b)
Closed and
===Discussed===
===Discussed===
 
None LIST OF ACRONYMS USED ADAMS Agencywide Documents Access and Management System CFR Code of Federal Regulations LCO Limiting Condition for Operation NRC U.S. Nuclear Regulatory Commission PARS Publicly Available Records System RHR Residual Heat Removal TS Technical Specifications  
None LIST OF ACRONYMS USED ADAMS         Agencywide Documents Access and Management System CFR           Code of Federal Regulations LCO           Limiting Condition for Operation NRC           U.S. Nuclear Regulatory Commission PARS           Publicly Available Records System RHR           Residual Heat Removal TS             Technical Specifications


==LIST OF DOCUMENTS REVIEWED==
==LIST OF DOCUMENTS REVIEWED==


}}
}}

Latest revision as of 00:42, 10 January 2025

Evaluations of Changes, Tests, and Experiments and Permanent Plant Modifications Baseline Inspection Report 05000263/2016008 (Reissuance)(Akd)
ML16118A261
Person / Time
Site: Monticello Xcel Energy icon.png
Issue date: 04/26/2016
From: Robert Daley
Engineering Branch 3
To: Gardner P
Northern States Power Co
References
IR 2016008
Download: ML16118A261 (13)


Text

April 26, 2016

SUBJECT:

MONTICELLO NUCLEAR GENERATING PLANT - EVALUATIONS OF CHANGES, TESTS, AND EXPERIMENTS AND PERMANENT PLANT MODIFICATIONS BASELINE INSPECTION REPORT 05000263/2016008

Dear Mr. Gardner:

On March 24, 2016, the U.S. Nuclear Regulatory Commission (NRC) completed an Evaluations of Changes, Tests, and Experiments and Permanent Plant Modifications inspection at your Monticello Nuclear Generating Plant. The enclosed inspection report documents the inspection results which were discussed on March 24, 2016, with Mr. M. Lingenfelter and other members of your staff.

The original report contained minor errors in Sections 1R17.1a and 1R17.2a concerning the documentation and completions of inspection samples, which are corrected in the inspection report enclosed with this letter.

The inspection examined activities conducted under your license as they relate to safety and compliance with the Commissions rules and regulations and with the conditions of your license.

The inspectors reviewed selected procedures and records, observed activities, and interviewed personnel.

No findings were identified during this inspection.

In accordance with Title 10 of the Code of Federal Regulations (10 CFR) 2.390, Public Inspections, Exemptions, Requests for Withholding, of the NRC's "Rules of Practice," a copy of this letter, its enclosure, and your response (if any) will be available electronically for public inspection in the NRCs Public Document Room or from the Publicly Available Records (PARS) component of the NRC's Agencywide Documents Access and Management System (ADAMS).

ADAMS is accessible from the NRC Web site at http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room).

Sincerely,

/RA Dariusz Szwarc Acting for

Robert C. Daley, Chief Engineering Branch 3 Division of Reactor Safety Docket No. 50-263 License No. DPR-22

Enclosure:

IR 05000263/2016008

REGION III==

Docket No:

50-263 License No:

DPR-22 Report No:

05000263/2016008 Licensee:

Northern States Power Company, Minnesota Facility:

Monticello Nuclear Generating Plant Location:

Monticello, MN Dates:

February 29 thru March 24, 2016 Inspectors:

Alan Dahbur, Senior Reactor Inspector (Lead)

Jorge J. Corujo-Sandín, Reactor Inspector Michael A. Jones, Reactor Inspector Approved by:

Robert C. Daley, Chief Engineering Branch 3 Division of Reactor Safety

SUMMARY

Inspection Report 05000263/2016008; 02/29/2016 - 03/24/2016; Monticello Nuclear Generating

Plant; Evaluations of Changes, Tests, and Experiments and Permanent Plant Modifications.

This report covers a 2-week announced baseline inspection on evaluations of changes, tests, and experiments and permanent plant modifications. The inspection was conducted by Region III based engineering inspectors. The U.S. Nuclear Regulatory Commissions program for overseeing the safe operation of commercial nuclear power reactors is described in NUREG-1649, Reactor Oversight Process, Revision 5, dated February 201

NRC-Identified

and Self-Revealed Findings No findings were identified.

Licensee-Identified Violations

No violations were identified.

REPORT DETAILS

REACTOR SAFETY

Cornerstones: Initiating Events, Mitigating Systems, and Barrier Integrity

1R17 Evaluations of Changes, Tests, and Experiments and Permanent Plant Modifications

.1 Evaluation of Changes, Tests, and Experiments

a. Inspection Scope

The inspectors reviewed 4 safety evaluations performed pursuant to Title 10, Code of Federal Regulations (CFR), Part 50, Section 59, to determine if the evaluations were adequate, and that prior U.S. Nuclear Regulatory Commission (NRC) approval was obtained as appropriate. The inspectors also reviewed 13 screenings where licensee personnel had determined that a 10 CFR 50.59 evaluation was not necessary. The inspectors reviewed these documents to determine if:

the changes, tests, and experiments performed were evaluated in accordance with 10 CFR 50.59 and that sufficient documentation existed to confirm that a license amendment was not required;

the safety issue requiring the change, tests or experiment was resolved;

the licensee conclusions for evaluations of changes, tests, and experiments were correct and consistent with 10 CFR 50.59; and

the design and licensing basis documentation was updated to reflect the change.

The inspectors used, in part, Nuclear Energy Institute Document 96-07, Guidelines for 10 CFR 50.59 Implementation, Revision 1, to determine acceptability of the completed evaluations, and screenings. The Nuclear Energy Institute document was endorsed by the NRC in Regulatory Guide 1.187, Guidance for Implementation of 10 CFR 50.59, Changes, Tests, and Experiments, dated November 2000. The inspectors also consulted Part 9900 of the NRC Inspection Manual, 10 CFR Guidance for 10 CFR 50.59, Changes, Tests, and Experiments.

This inspection constituted 4 samples of evaluations and 13 samples of screenings and/or applicability determinations as defined in Inspection Procedure 71111.17-04.

b. Findings

(Open) Unresolved Item 05000263/2016008-01, Failure to provide acceptable Alternate Methods of Decay Heat Removal

Introduction:

The inspectors identified an Unresolved Item associated with Technical Specification (TS) 3.4.8, Residual Heat Removal (RHR) Shutdown Cooling System - Cold Shutdown. Specifically, the licensee failed to verify that the capability of the alternate methods of decay heat removal described in Operations Manual C.4-B.03.04.A, Loss of Normal Shutdown Cooling, were adequate to combat a loss of shutdown cooling resulting from the loss of one or two RHR subsystems while in MODE 4 with high decay heat load.

Description:

The Limiting Condition for Operation (LCO) 3.4.8 of TS Residual Heat Removal Shutdown Cooling System - Cold Shutdown, required in Mode 4, two RHR shutdown cooling subsystems shall be operable, and, with no recirculation pump in operation, at least one RHR shutdown cooling subsystem shall be in operation. The TS Bases Section 3.4.8, indicated that an operable RHR shutdown cooling subsystem consisted of one operable RHR pump, one heat exchanger, the associated piping and valves, and the necessary portions of the RHR Service Water System System capable of providing cooling water to the heat exchanger. The TS Bases Section 3.4.8 further indicated that the two subsystems have a common suction source and were allowed to have a common heat exchanger and common discharge piping. Thus, to meet the LCO, both pumps in one loop or one pump in each of the two loops must be operable. Since the piping and heat exchangers were passive components that were assumed not to fail, they were allowed to be common to both subsystems.

When TS 3.4.8, LCO could not be met, Condition A, for one or two RHR shutdown cooling subsystems inoperable, the Required Action was to, verify an alternate method of decay heat removal was available for each inoperable RHR shutdown cooling subsystem. The completion time for the required action was 1 hour1.157407e-5 days <br />2.777778e-4 hours <br />1.653439e-6 weeks <br />3.805e-7 months <br />, and once per 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> thereafter. The TS Bases 3.4.8 for Condition A indicated that with one of the two required RHR shutdown cooling subsystems inoperable, the remaining subsystem was capable of providing the required decay heat removal. However, the overall reliability was reduced, therefore, an alternate method of decay heat removal must be provided. With both RHR shutdown cooling subsystems inoperable, an alternate method of decay heat removal must be provided in addition to that provided for the initial RHR shutdown cooling subsystem inoperability. This was to ensure the re-establishment of backup decay heat removal capabilities, similar to the requirements of the LCO. The bases further stated that the required cooling capacity of the alternate method should be ensured by verifying (by calculation or demonstration) its capability to maintain or reduce temperature. Alternate methods that can be used included (but not limited to) the Reactor Water Cleanup System by itself or using feed and bleed in combination with Control Rod Drive System or Condensate/Feed Systems.

Abnormal Procedure, Operations Manual C.4-B.03.04.A, Loss of Normal Shutdown Cooling, provided instructions for establishing alternate methods for decay heat removal. The inspectors noticed that except for the alternate method as described below in the G-EK-1-45, the licensee was not able to show by calculation or demonstration that the systems and methods credited in this procedure would be capable of providing sufficient heat removal capability or appropriate levels of redundancy as required by TS 3.4.8.

The G-EK-1-45 was a General Electric Letter to Northern States Power, Subject: Cold Shutdown Capability Report, dated April 22, 1981. This letter provided a report which described the capability of the Monticello Nuclear Generating Plant to achieve cold shutdown using only safety class systems and assuming the worst single failure. The alternate shutdown decay heat removal method used in the report credited combinations of the RHR pumps and heat exchangers in the suppression pool cooling mode of RHR to ensure suppression pool water temperatures were below the design limit. This method utilized the core spray system and safety relief valves to circulate reactor inventory to remove decay heat from the reactor.

The inspectors noted that calculations supporting the above alternate strategy utilized an RHR subsystem that could be inoperable and/or unavailable and therefore may not be credited to comply with TS 3.4.8. Specifically, the inspectors were concerned that while the plant was in mode 4, with a credited one subsystem inoperable, the licensees credited alternate decay heat removal method that relied on an RHR subsystem, to perform the required suppression pool cooling function. The inspectors were concerned that relying on the only operable RHR subsystem for the alternate method did not meet the intent of the TS requirement as described in the TS Bases. Furthermore, the inspectors noticed for Mode 4 with two RHR subsystems inoperable, the licensee failed to verify by calculation or demonstrations that two additional redundant alternate decay heat removal methods existed with sufficient capacity to maintain the average reactor coolant temperature below 212 degrees Fahrenheit.

During the inspection, the licensee indicated that the Boiling Reactor Owners Group was in the process of developing a draft TS Task Force Traveler to address the requirement of TS 3.4.8 and its Bases.

Based on the information above, the inspectors were concerned that the plant Operations Manual was inadequate and failed to include alternate decay heat removal methods that would enable the licensee to comply with the requirement of TS 3.4.8. The Operations Manual was required per TS 5.4.1, Procedures, which required that written procedures shall be established, implemented, and maintained covering the emergency operating procedures. The inspectors determined that this issue was unresolved pending the actions by the licensee and the Boiling Reactor Owners Group and the NRC review of these actions. The licensee entered the inspectors concerns into their Corrective Action Program as AR 01516098. (URI 05000263/2016008-01, Failure to Provide Acceptable Alternate Methods of Decay Heat Removal)

.2 Permanent Plant Modifications

a. Inspection Scope

The inspectors reviewed 8 permanent plant modifications that had been installed in the plant during the last 3 years. This review included in-plant walkdowns portions of the high-pressure coolant injection steam drain line system, the Emergency Diesel Generator Fuel Oil Transfer System, including the Diesel Fuel Oil pump house, the new diesel fuel oil pumps installed in the day tank room, and portions of the fuel oil storage tank tornado missile protection modifications. The modifications were selected based upon risk significance, safety significance, and complexity. The inspectors reviewed the modifications selected to determine if:

the supporting design and licensing basis documentation was updated;

the changes were in accordance with the specified design requirements;

the procedures and training plans affected by the modification have been adequately updated;

the test documentation as required by the applicable test programs has been updated; and

post-modification testing adequately verified system operability and/or functionality.

The inspectors also used applicable industry standards to evaluate acceptability of the modifications. The list of modifications and other documents reviewed by the inspectors is included as an Attachment to this report.

This inspection constituted eight permanent plant modification samples as defined in Inspection Procedure 71111.17-04.

OTHER ACTIVITIES

4OA2 Problem Identification and Resolution

.1 Routine Review of Condition Reports

a. Inspection Scope

The inspectors reviewed several corrective action process documents that identified or were related to Title 10 of the Code of Federal Regulations, Part 50.59 evaluations and permanent plant modifications. The inspectors reviewed these documents to evaluate the effectiveness of corrective actions related to permanent plant modifications and evaluations of changes, tests, and experiments. In addition, corrective action documents written on issues identified during the inspection were reviewed to verify adequate problem identification and incorporation of the problems into the corrective action system. The specific corrective action documents that were sampled and reviewed by the inspectors are listed in the attachment to this report.

b. Findings

No findings were identified.

4OA6 Management Meetings

.1

Exit Meeting Summary

On March 24, 2016, the inspectors presented the inspection results to Mr. M. Lingenfelter, and other members of the licensee staff. The licensee personnel acknowledged the inspection results presented and did not identify any proprietary content. The inspectors confirmed that all proprietary material provided to the inspection team was identified and will be dispositioned in accordance with applicable processes.

ATTACHMENT:

SUPPLEMENTAL INFORMATION

KEY POINTS OF CONTACT

Licensee

M. Lingenfelter, Director of Engineering
A. Gonnering, Design Engineering
M. Kelly, Performance Assurance Manager
J. Gausman, Engineering
A. Ward, Regulatory Affairs Manager
T. Hurrle, Design Engineering Manager
B. Halvorson, Engineering
A. Kouba, Regulatory Affairs
D. Alstad, Design Engineer
E. Watzel, Electrical Design Engineering Supervisor

U.S. Nuclear Regulatory Commission

P. Zurawski, Senior Resident Inspector
P. LaFlamme, Acting Senior Resident Inspector
D. Krause, Resident Inspector

LIST OF ITEMS

OPENED, CLOSED AND DISCUSSED

Opened

05000263/2016008-01 URI Failure to provide acceptable Alternate Methods of Decay Heat Removal (Section 1R17.1b)

Closed and

Discussed

None LIST OF ACRONYMS USED ADAMS Agencywide Documents Access and Management System CFR Code of Federal Regulations LCO Limiting Condition for Operation NRC U.S. Nuclear Regulatory Commission PARS Publicly Available Records System RHR Residual Heat Removal TS Technical Specifications

LIST OF DOCUMENTS REVIEWED