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=Text=
=Text=
{{#Wiki_filter:uly 23, 2019
{{#Wiki_filter:July 23, 2019


==SUBJECT:==
==SUBJECT:==
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Sincerely,
Sincerely,
/RA/
/RA/  
Omar R. López-Santiago, Chief Reactor Projects Branch 5 Division of Reactor Projects Docket Nos.: 05000327 and 05000328 License Nos.: DPR-77 and DPR-79
 
Omar R. López-Santiago, Chief Reactor Projects Branch 5 Division of Reactor Projects  
 
Docket Nos.: 05000327 and 05000328 License Nos.: DPR-77 and DPR-79  


===Enclosure:===
===Enclosure:===
As stated
As stated  


==Inspection Report==
==Inspection Report==
Docket Numbers: 05000327 and 05000328 License Numbers: DPR-77 and DPR-79 Report Numbers: 05000327/2019011 and 05000328/2019011 Enterprise Identifier: I-2019-011-0036 Licensee: Tennessee Valley Authority Facility: Sequoyah Nuclear Plant, Units 1 and 2 Location: Soddy-Daisy, TN 37379 Inspection Dates: June 03, 2019 to June 27, 2019 Inspectors: J. Seat, Project Engineer M. Checkle, Senior Allegations Coordinator N. Childs, Resident Inspector W. Deschaine, Project Engineer Approved By: Omar R. López-Santiago, Chief Reactor Projects Branch 5 Division of Reactor Projects Enclosure
Docket Numbers:
05000327 and 05000328  
 
License Numbers:
DPR-77 and DPR-79  
 
Report Numbers:
05000327/2019011 and 05000328/2019011  
 
Enterprise Identifier: I-2019-011-0036  
 
Licensee:
Tennessee Valley Authority  
 
Facility:
Sequoyah Nuclear Plant, Units 1 and 2  
 
Location:
Soddy-Daisy, TN 37379  
 
Inspection Dates:
June 03, 2019 to June 27, 2019  
 
Inspectors:
J. Seat, Project Engineer  
 
M. Checkle, Senior Allegations Coordinator  
 
N. Childs, Resident Inspector  
 
W. Deschaine, Project Engineer  
 
Approved By:
Omar R. López-Santiago, Chief
Reactor Projects Branch 5
Division of Reactor Projects  


=SUMMARY=
=SUMMARY=
The U.S. Nuclear Regulatory Commission (NRC) continued monitoring the licensees performance by conducting a biennial problem identification and resolution inspection at Sequoyah Nuclear Plant, Units 1 and 2, in accordance with the Reactor Oversight Process. The Reactor Oversight Process is the NRCs program for overseeing the safe operation of commercial nuclear power reactors. Refer to https://www.nrc.gov/reactors/operating/oversight.html for more information.
The U.S. Nuclear Regulatory Commission (NRC) continued monitoring the licensees performance by conducting a biennial problem identification and resolution inspection at Sequoyah Nuclear Plant, Units 1 and 2, in accordance with the Reactor Oversight Process. The Reactor Oversight Process is the NRCs program for overseeing the safe operation of commercial nuclear power reactors. Refer to https://www.nrc.gov/reactors/operating/oversight.html for more information.


List of Findings and Violations Failure to Adequately Implement Requirements of Confirmatory Order EA-17-022,
===List of Findings and Violations===
Commitment V.1.b.3 Cornerstone         Significance                             Cross-Cutting       Report Aspect              Section Not Applicable       NCV 05000327,05000328/2019011-           Not Applicable      92702
Failure to Adequately Implement Requirements of Confirmatory Order EA-17-022,
Commitment V.1.b.3 Cornerstone Significance Cross-Cutting Aspect Report Section Not Applicable NCV 05000327,05000328/2019011-


Open/Closed The inspectors identified a Severity Level IV NCV for the licensees failure to adequately implement requirements of Confirmatory Order (CO) EA-17-022, Commitment V.1.b.3. Specifically, the licensee failed to ensure that new supervisory employees completed safety conscious work environment (SCWE) training within three months of their hire or promotion effective date.
Open/Closed Not Applicable 92702 The inspectors identified a Severity Level IV NCV for the licensees failure to adequately implement requirements of Confirmatory Order (CO) EA-17-022, Commitment V.1.b.3. Specifically, the licensee failed to ensure that new supervisory employees completed safety conscious work environment (SCWE) training within three months of their hire or promotion effective date.


Additional Tracking Items None
===Additional Tracking Items===
None


=INSPECTION SCOPES=
=INSPECTION SCOPES=
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==OTHER ACTIVITIES - BASELINE==
==OTHER ACTIVITIES - BASELINE==
===71152B - Problem Identification and Resolution Biennial Team Inspection (IP Section 02.04)===
{{IP sample|IP=IP 71152|count=1}}


===71152B - Problem Identification and Resolution Biennial Team Inspection (IP Section 02.04) ===
{{IP sample|IP=IP 71152|count=1}}
The inspectors performed a biennial assessment of the licensees corrective action program, use of operating experience, self-assessments and audits, and safety conscious work environment.
The inspectors performed a biennial assessment of the licensees corrective action program, use of operating experience, self-assessments and audits, and safety conscious work environment.
* Corrective Action Program Effectiveness: The inspectors assessed the corrective action programs effectiveness in identifying, prioritizing, evaluating, and correcting problems.
* Corrective Action Program Effectiveness: The inspectors assessed the corrective action programs effectiveness in identifying, prioritizing, evaluating, and correcting problems.
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==OTHER ACTIVITIES==
==OTHER ACTIVITIES==
- TEMPORARY INSTRUCTIONS, INFREQUENT AND ABNORMAL
- TEMPORARY INSTRUCTIONS, INFREQUENT AND ABNORMAL  


===92702 CONF - Enforcement Related Order Follow-Up-Only Enforcement Related Order Follow-Up-Only ===
===92702 CONF - Enforcement Related Order Follow-Up-Only Enforcement Related Order Follow-Up-Only===
{{IP sample|IP=IP 92702|count=1}}
{{IP sample|IP=IP 92702|count=1}}
The inspectors reviewed commitments associated with four items from Confirmatory Order EA-17-022, issued to TVA on July 27, 2017.
The inspectors reviewed commitments associated with four items from Confirmatory Order EA-17-022, issued to TVA on July 27, 2017.
: (1) Commitment V.1.b.2: This commitment and action required that training be provided within one year and on an annual basis thereafter to, at a minimum, all working status nuclear business group supervisory employees, contractor supervisory employees involved in nuclear-related work activities, human resource staff involved in the adverse employment action process, employee concerns program staff, contract technical stewards for nuclear-related work activities, and the personnel in the TVA Office of General Counsel who are engaged in nuclear-related work activities. TVA identified 419 individuals at Sequoyah and TVA Corporate who were required to complete the training. The inspectors verified that the list of individuals included first line supervisors and above, contract technical stewards, human resources personnel, and employee concerns program personnel. The inspection was only completed for Sequoyah and TVA Corporate.
: (1) Commitment V.1.b.2: This commitment and action required that training be provided within one year and on an annual basis thereafter to, at a minimum, all working status nuclear business group supervisory employees, contractor supervisory employees involved in nuclear-related work activities, human resource staff involved in the adverse employment action process, employee concerns program staff, contract technical stewards for nuclear-related work activities, and the personnel in the TVA Office of General Counsel who are engaged in nuclear-related work activities. TVA identified 419 individuals at Sequoyah and TVA Corporate who were required to complete the training. The inspectors verified that the list of individuals included first line supervisors and above, contract technical stewards, human resources personnel, and employee concerns program personnel. The inspection was only completed for Sequoyah and TVA Corporate.
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==INSPECTION RESULTS==
==INSPECTION RESULTS==
Assessment                                                                               71152B 1. Corrective Action Program Effectiveness Based on the samples reviewed, the team determined that the licensees corrective action program (CAP) complied with regulatory requirements and self-imposed standards. The licensees implementation of the CAP adequately supported nuclear safety.
Assessment 71152B  
 
===1. Corrective Action Program Effectiveness===
Based on the samples reviewed, the team determined that the licensees corrective action program (CAP) complied with regulatory requirements and self-imposed standards. The licensees implementation of the CAP adequately supported nuclear safety.


Problem Identification: The team determined that most conditions that required generation of a condition report (CR) by licensee procedure, NPG-SPP-22.300, Corrective Action Program, had been appropriately entered into the CAP. The team observed members at the Management Review Committee (MRC) and Plant Screening Committee (PSC) meetings appropriately questioning and challenging condition reports to ensure clarification of issues and appropriate entry into the CAP. Based on the samples reviewed, the team determined that the licensee trended equipment and programmatic issues, and appropriately identified problems in condition reports. Additionally, the team concluded that personnel were identifying trends at low levels. The inspectors performed walkdowns, reviewed CRs, and reviewed system health and trending reports for the Auxiliary Feedwater System (AFW) and Chemical and Volume Control System (CVCS). Based on the inspectors' reviews and walkdowns of accessible portions of those systems, the inspectors determined that deficiencies were being identified and placed in the CAP. Overall, the team determined that the licensee is identifying problems at the proper threshold and entering them into the corrective action program.
Problem Identification: The team determined that most conditions that required generation of a condition report (CR) by licensee procedure, NPG-SPP-22.300, Corrective Action Program, had been appropriately entered into the CAP. The team observed members at the Management Review Committee (MRC) and Plant Screening Committee (PSC) meetings appropriately questioning and challenging condition reports to ensure clarification of issues and appropriate entry into the CAP. Based on the samples reviewed, the team determined that the licensee trended equipment and programmatic issues, and appropriately identified problems in condition reports. Additionally, the team concluded that personnel were identifying trends at low levels. The inspectors performed walkdowns, reviewed CRs, and reviewed system health and trending reports for the Auxiliary Feedwater System (AFW) and Chemical and Volume Control System (CVCS). Based on the inspectors' reviews and walkdowns of accessible portions of those systems, the inspectors determined that deficiencies were being identified and placed in the CAP. Overall, the team determined that the licensee is identifying problems at the proper threshold and entering them into the corrective action program.
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===2. Use of Operating Experience (OE)===
===2. Use of Operating Experience (OE)===
Based on a review of selected documentation related to operating experience issues, the team determined that the licensee was generally effective in screening industry and NRC OE for applicability to the plant. Industry OE was evaluated at either the corporate or plant level depending on the source and type of document. Relevant information was forwarded to the applicable department for further action or informational purposes. Operating experience issues requiring action were entered into the CAP for tracking and closure. The team determined that the licensee's use of industry and NRC OE was effective, and the program adequately supported nuclear safety. The team did note that procedural requirements related to OE screening timeliness were vague, however, the team did not identify any instances where OE was not screened in a timely manner.
Based on a review of selected documentation related to operating experience issues, the team determined that the licensee was generally effective in screening industry and NRC OE for applicability to the plant. Industry OE was evaluated at either the corporate or plant level depending on the source and type of document. Relevant information was forwarded to the applicable department for further action or informational purposes. Operating experience issues requiring action were entered into the CAP for tracking and closure. The team determined that the licensee's use of industry and NRC OE was effective, and the program adequately supported nuclear safety. The team did note that procedural requirements related to OE screening timeliness were vague, however, the team did not identify any instances where OE was not screened in a timely manner.


===3. Self-Assessments and Audits===
===3. Self-Assessments and Audits===
The team determined that the scopes of assessments and audits were adequate. Self-assessments were generally detailed and critical. The team verified that CRs were created to document areas for improvement and findings resulting from self-assessments, and verified that actions had been completed consistent with those recommendations. Audits of the quality assurance program appropriately assessed performance and identified areas for improvement. Generally, the licensee performed evaluations that were technically accurate.
The team determined that the scopes of assessments and audits were adequate. Self-assessments were generally detailed and critical. The team verified that CRs were created to document areas for improvement and findings resulting from self-assessments, and verified that actions had been completed consistent with those recommendations. Audits of the quality assurance program appropriately assessed performance and identified areas for improvement. Generally, the licensee performed evaluations that were technically accurate.


===4. Safety Conscious Work Environment===
===4. Safety Conscious Work Environment===
Based on a sample size of approximately 35 individuals, interviewed from a cross-section of plant employees at Sequoyah and the TVA Corporate office, the team found no evidence of challenges to a safety-conscious work environment at either location. The following departments were sampled: Nuclear Oversight - Quality Assurance (52% sample),
Based on a sample size of approximately 35 individuals, interviewed from a cross-section of plant employees at Sequoyah and the TVA Corporate office, the team found no evidence of challenges to a safety-conscious work environment at either location. The following departments were sampled: Nuclear Oversight - Quality Assurance (52% sample),
Maintenance (12% sample), Chemistry (6% sample), Radiation Protection (8% sample),
Maintenance (12% sample), Chemistry (6% sample), Radiation Protection (8% sample),
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* Do you feel like you are able to be open when participating in ECP pulsing surveys or other work environment assessments?
* Do you feel like you are able to be open when participating in ECP pulsing surveys or other work environment assessments?
* Are you aware of the proposed changes regarding the ECP program at TVA?
* Are you aware of the proposed changes regarding the ECP program at TVA?
* Do you feel like the new ECP structure would still provide independence from management?
* Do you feel like the new ECP structure would still provide independence from management?  
 
Prior to the inspection, the licensee made fleet-wide communications regarding proposed changes to the ECP. When queried about the proposed ECP changes during the interviews, 31% of those interviewees were concerned that the proposed structure of the ECP would not provide independence from management, however, most would still be willing to use the ECP.
Prior to the inspection, the licensee made fleet-wide communications regarding proposed changes to the ECP. When queried about the proposed ECP changes during the interviews, 31% of those interviewees were concerned that the proposed structure of the ECP would not provide independence from management, however, most would still be willing to use the ECP.


Minor Violation                                                                         71152B Minor Violation: 10 CFR 50, Appendix B, Criterion V, "Instructions, Procedures, and Drawings," states, in part, "Activities affecting quality shall be prescribed by documented instructions, procedures, or drawings, of a type appropriate to the circumstances and shall be accomplished in accordance with these instructions, procedures, or drawings."
Minor Violation 71152B Minor Violation: 10 CFR 50, Appendix B, Criterion V, "Instructions, Procedures, and Drawings," states, in part, "Activities affecting quality shall be prescribed by documented instructions, procedures, or drawings, of a type appropriate to the circumstances and shall be accomplished in accordance with these instructions, procedures, or drawings."


Contrary to the above, on August 15, 2017, the licensee failed to accomplish activities affecting quality in accordance with established procedures. Specifically, the licensee did not follow procedure NPG-SPP-22.300, "Corrective Action Program," Revision 9, step 3.7.6.B.1, which requires that corrective action controls (CA Control Flag in Maximo) be applied to work orders (WOs) credited for closure of a condition report requiring corrective actions. CR 1313355, which documented undersized seismic restraints securing temporary equipment, was closed to WO 118888040 without applying the required corrective action controls. WO 118888040 was later closed without sufficient evidence to demonstrate that appropriate actions had been taken to correct the condition identified in CR 1313355. The failure to apply corrective action controls to WO 118888040, per NPG-SPP-22.300, was a performance deficiency.
Contrary to the above, on August 15, 2017, the licensee failed to accomplish activities affecting quality in accordance with established procedures. Specifically, the licensee did not follow procedure NPG-SPP-22.300, "Corrective Action Program," Revision 9, step 3.7.6.B.1, which requires that corrective action controls (CA Control Flag in Maximo) be applied to work orders (WOs) credited for closure of a condition report requiring corrective actions. CR 1313355, which documented undersized seismic restraints securing temporary equipment, was closed to WO 118888040 without applying the required corrective action controls. WO 118888040 was later closed without sufficient evidence to demonstrate that appropriate actions had been taken to correct the condition identified in CR 1313355. The failure to apply corrective action controls to WO 118888040, per NPG-SPP-22.300, was a performance deficiency.
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The licensee initiated CR 1526428 to address this minor violation. The licensee performed walkdowns to verify that temporary equipment secured with undersized seismic restraints was no longer present. This failure to comply with procedural requirements constitutes a minor violation that is not subject to enforcement action in accordance with the NRCs Enforcement Policy.
The licensee initiated CR 1526428 to address this minor violation. The licensee performed walkdowns to verify that temporary equipment secured with undersized seismic restraints was no longer present. This failure to comply with procedural requirements constitutes a minor violation that is not subject to enforcement action in accordance with the NRCs Enforcement Policy.


Failure to Adequately Implement Requirements of Confirmatory Order EA-17-022, Commitment V.1.b.3 Cornerstone       Severity                                           Cross-Cutting Report Aspect        Section Not               Severity Level IV                                 Not            92702 Applicable        NCV 05000327,05000328/2019011-01                   Applicable Open/Closed The inspectors identified a Severity Level (SL) IV NCV for the licensees failure to adequately implement requirements of Confirmatory Order EA-17-022, Commitment V.1.b.3. Specifically, the licensee failed to ensure that new supervisory employees completed safety conscious work environment (SCWE) training within three months of their hire or promotion effective date.
Failure to Adequately Implement Requirements of Confirmatory Order EA-17-022, Commitment V.1.b.3 Cornerstone Severity Cross-Cutting Aspect Report Section Not Applicable Severity Level IV NCV 05000327,05000328/2019011-01 Open/Closed  
 
Not Applicable 92702 The inspectors identified a Severity Level (SL) IV NCV for the licensees failure to adequately implement requirements of Confirmatory Order EA-17-022, Commitment V.1.b.3. Specifically, the licensee failed to ensure that new supervisory employees completed safety conscious work environment (SCWE) training within three months of their hire or promotion effective date.


=====Description:=====
=====Description:=====
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Corrective Actions: The licensee entered this issue into their corrective action program on December 26, 2018 and took immediate action to ensure all Sequoyah employees had completed the training by February 6, 2019. A CR was written on December 26, 2018, with actions to perform an apparent cause analysis of the incorrect due dates and track actions at the TVA Corporate level. The licensee initiated a CR on March 5, 2019, to document the missed SCWE training for new contractor supervisory employees.
Corrective Actions: The licensee entered this issue into their corrective action program on December 26, 2018 and took immediate action to ensure all Sequoyah employees had completed the training by February 6, 2019. A CR was written on December 26, 2018, with actions to perform an apparent cause analysis of the incorrect due dates and track actions at the TVA Corporate level. The licensee initiated a CR on March 5, 2019, to document the missed SCWE training for new contractor supervisory employees.


Corrective Action References: CR 1477482, CR 1477964, CR 1484364, CR 1478023, CR 1497144
Corrective Action References: CR 1477482, CR 1477964, CR 1484364, CR 1478023, CR 1497144  


=====Performance Assessment:=====
=====Performance Assessment:=====
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=DOCUMENTS REVIEWED=
=DOCUMENTS REVIEWED=


Inspection Type             Designation         Description or Title                               Revision or
Inspection
Procedure                                                                                            Date
Procedure
71152B     Calculations     MDQ0000682018000101 Material Aging for PORV Target Rock Solenoid Valves Revision 0
Type
                                                  (SQNEQ-SOL-002)
Designation
71152B     Calculations     SCG1S596           Maintenance Rule for Structures and License Renewal Revision 13
Description or Title
Revision or
Date
71152B
Calculations
MDQ0000682018000101 Material Aging for PORV Target Rock Solenoid Valves  
(SQNEQ-SOL-002)
Revision 0
71152B
Calculations
SCG1S596
Maintenance Rule for Structures and License Renewal
Structures Monitoring Program Inspections
Structures Monitoring Program Inspections
71152B     Corrective Action CR 1002259         OE - Foreign Material Damages Steam Generator       03/20/2015
Revision 13
Documents                            Tube Sheet
71152B
71152B    Corrective Action CR 1002268         OE - Performance Shortfalls During Mechanical       03/20/2015
Corrective Action
Documents                            Maintenance Activities
Documents
71152B    Corrective Action CR 1002270         NOER - Loss of Breaker Configuration Control PER   03/20/2015
CR 1002259
Documents                            965728
OE - Foreign Material Damages Steam Generator
71152B    Corrective Action CR 1002275         NOER - Missed Surveillance on New Components       03/20/2015
Tube Sheet
03/20/2015
71152B
Corrective Action
Documents
CR 1002268
OE - Performance Shortfalls During Mechanical
Maintenance Activities
03/20/2015
71152B
Corrective Action
Documents
CR 1002270
NOER - Loss of Breaker Configuration Control PER
965728
03/20/2015
71152B
Corrective Action
Documents
CR 1002275
NOER - Missed Surveillance on New Components
03/20/2015
71152B
Corrective Action
Documents
Documents
71152B    Corrective Action CR 1002293         OE - Loss of Jet Pump Plug Seals in Reactor Vessel 03/20/2015
CR 1002293
OE - Loss of Jet Pump Plug Seals in Reactor Vessel
03/20/2015
71152B
Corrective Action
Documents
Documents
71152B    Corrective Action CR 1003153         OE - BFN Loss of Inventory from Reactor Cavity     03/23/2015
CR 1003153
OE - BFN Loss of Inventory from Reactor Cavity
03/23/2015
71152B
Corrective Action
Documents
Documents
71152B    Corrective Action CR 1017143         Found Cracks in the Cover on Vital Battery #2       04/22/2015
CR 1017143
Found Cracks in the Cover on Vital Battery #2
04/22/2015
71152B
Corrective Action
Documents
Documents
71152B    Corrective Action CR 1023172         NOER - Reactor Trip due to Loss of Main Condenser   05/07/2015
CR 1023172
Documents                            Vacuum
NOER - Reactor Trip due to Loss of Main Condenser
71152B    Corrective Action CR 1023175          NOER - PER Classification and Level of Significance 05/07/2015
Vacuum
05/07/2015
71152B
Corrective Action
Documents
Documents
71152B    Corrective Action CR 1023207          OE - Ice Bed Increasing Temperature Trends          05/07/2015
CR 1023175
NOER - PER Classification and Level of Significance
05/07/2015
71152B
Corrective Action
Documents
Documents
71152B    Corrective Action CR 1025764          Oil Bubbler is at 20% Recommend Minor Maintenance  05/14/2015
CR 1023207
Documents                            to Fill Reservoir
OE - Ice Bed Increasing Temperature Trends
71152B    Corrective Action CR 1064736          Evaluate DCN 23085 - Kirk Key Interlocks            07/30/2015
05/07/2015
71152B
Corrective Action
Documents
Documents
71152B    Corrective Action CR 1084294          NRC NCV 2015-007-02 - 50.59/Modifications          09/21/2015
CR 1025764
Documents                            Inspection
Oil Bubbler is at 20% Recommend Minor Maintenance
71152B    Corrective Action CR 1104335          CRDM Cable Connection Issues Found During          11/15/2015
to Fill Reservoir
Documents                            Disconnection
05/14/2015
Inspection Type              Designation Description or Title                              Revision or
71152B
Procedure                                                                                  Date
Corrective Action
71152B    Corrective Action CR 1106765  1-LCV-3-148 not Able to be Operated in Manual      11/20/2015
Documents
Documents
71152B    Corrective Action CR 1116558  2-FSV-43-55 Failed 2-SI-SXV-000-204.0 Valve Stroke 12/16/2015
CR 1064736
Evaluate DCN 23085 - Kirk Key Interlocks
07/30/2015
71152B
Corrective Action
Documents
Documents
71152B    Corrective Action CR 1121723  2-FSV-43-61 Has no Light Indication While Valve is 01/05/2016
CR 1084294
Documents                    Closed
NRC NCV 2015-007-02 - 50.59/Modifications
71152B    Corrective Action CR 115765  Potential Transformer (PT) in Compartment #3      12/01/2006
Inspection
09/21/2015
71152B
Corrective Action
Documents
Documents
71152B    Corrective Action CR 1169090  Post Accident Monitoring (2-XX-55-6L) for Valve 2- 05/09/2016
CR 1104335
Documents                    FCV-43-61 Indicates Intermediate Position
CRDM Cable Connection Issues Found During
71152B    Corrective Action CR 1181710  NRC CDBI DG Bldg Ventilation System and Tornado    06/14/2016
Disconnection
Documents                    Impact
11/15/2015
71152B    Corrective Action CR 1187308  Operations Request POE - Instrument Calibration    06/30/2016
 
Documents                    Issues
Inspection
71152B     Corrective Action CR 1227157  Potential Error Trap with Breaker UNIDs            10/26/2016
Procedure
Type
Designation
Description or Title
Revision or
Date
71152B
Corrective Action
Documents
Documents
71152B     Corrective Action CR 1240813 0-MI-MRR-003-461.0 Needs to be Revised - TDAFW     12/10/2016
CR 1106765
Documents                    Mech Overspeed Trip Linkage Spring Setting is
1-LCV-3-148 not Able to be Operated in Manual
11/20/2015
71152B
Corrective Action
Documents
CR 1116558
2-FSV-43-55 Failed 2-SI-SXV-000-204.0 Valve Stroke
2/16/2015
71152B
Corrective Action
Documents
CR 1121723
2-FSV-43-61 Has no Light Indication While Valve is
Closed
01/05/2016
71152B
Corrective Action
Documents
CR 115765
Potential Transformer (PT) in Compartment #3
2/01/2006
71152B
Corrective Action
Documents
CR 1169090
Post Accident Monitoring (2-XX-55-6L) for Valve 2-
FCV-43-61 Indicates Intermediate Position
05/09/2016
71152B
Corrective Action
Documents
CR 1181710
NRC CDBI DG Bldg Ventilation System and Tornado
Impact
06/14/2016
71152B
Corrective Action
Documents
CR 1187308
Operations Request POE - Instrument Calibration
Issues
06/30/2016
71152B
Corrective Action
Documents
CR 1227157
Potential Error Trap with Breaker UNIDs
10/26/2016
71152B
Corrective Action
Documents
CR 1240813
0-MI-MRR-003-461.0 Needs to be Revised - TDAFW
Mech Overspeed Trip Linkage Spring Setting is
Incorrect
Incorrect
71152B     Corrective Action CR 1254470 CRs Closed to WOs Without Correct Coding in WO     01/25/2017
2/10/2016
71152B
Corrective Action
Documents
CR 1254470
CRs Closed to WOs Without Correct Coding in WO
01/25/2017
71152B
Corrective Action
Documents
CR 1254937
NOER was not Generated for CR 1241933
01/26/2017
71152B
Corrective Action
Documents
CR 1255171
Gaps in Extent of Condition Review of QA Finding
RCA 1155352
01/26/2017
71152B
Corrective Action
Documents
CR 1255177
Trend in Site CAP Procedure Adherence to NPG-SPP-
2.300
01/26/2017
71152B
Corrective Action
Documents
CR 1269767
A212 ABSCE Breach Resulting in Both Trains of
ABGTS Inoperable for Both Units
03/07/2017
71152B
Corrective Action
Documents
CR 1290969
Snapshot Assessment - PD - SQN-PI-SSA-17-007 -
OE Coordinators
05/02/2017
71152B
Corrective Action
Documents
CR 1301718
Unit 1 TDAFW Suction Pressure Gauge Found
Isolated
05/30/2017
71152B
Corrective Action
CR 1303852
RP REP VANS
06/05/2017
 
Inspection
Procedure
Type
Designation
Description or Title
Revision or
Date
Documents
71152B
Corrective Action
Documents
CR 1305710
Procedure Change Request for 2-SI-SXV-003-219.S
06/10/2017
71152B
Corrective Action
Documents
CR 1311223
QA ID: The Chemical Hygiene Plan was not reviewed
during 2016 (SSA1707)
06/26/2017
71152B
Corrective Action
Documents
CR 1311501
QA ID: SSA1707: Inconsistent performance of
surveillance procedure requirements
06/27/2017
71152B
Corrective Action
Documents
CR 1313355
Inadequate chain size used for temporary equipment
seismic restraint
07/03/2017
71152B
Corrective Action
Documents
CR 1313866
OE-Green-WBN-NOER-17-014-Unplanned LCO 3.7.5
entry due to time delay relay failure
07/05/2017
71152B
Corrective Action
Documents
CR 1321168
Corrective Action for CR 1303852 did not resolve
condition identified
07/25/2017
71152B
Corrective Action
Documents
CR 1323549
QAID Improper use of N/A (SSA 1708)
08/01/2017
71152B
Corrective Action
Documents
CR 1323551
QA Records from ALARA not being transmitted to
EDMS
08/01/2017
71152B
Corrective Action
Documents
CR 1323555
QAID Temporary Shielding forms not properly filled out
(SSA 1708)
08/01/2017
71152B
Corrective Action
Documents
CR 1323558
QAID Recommendation on temporary shielding
support (SSA 1708)
08/01/2017
71152B
Corrective Action
Documents
CR 1324371
Follow-up on CR 1324282 from SQN RP - RW Audit
08/03/2017
71152B
Corrective Action
Documents
CR 1334122
NRC Regulatory Issue Summary (RIS) 2017-04
08/31/2017
71152B
Corrective Action
Documents
CR 1336290
Cable Tray Supports out of Tolerance
09/07/2017
71152B
Corrective Action
Documents
CR 1341686
Cable Tray Supports out of Tolerance
09/25/2017
71152B
Corrective Action
Documents
CR 1343410
SGI records
09/29/2017
71152B
Corrective Action
Documents
CR 1364616
OE - Part 21 2017-52-00 Fisher Type 461 Valve Plug
Machining
2/04/2017
71152B
Corrective Action
CR 1366082
SQN DBA EQ 201700X
2/07/2017
 
Inspection
Procedure
Type
Designation
Description or Title
Revision or
Date
Documents
71152B
Corrective Action
Documents
CR 1366200
Unit 1 Lower Compartment Cooler Motor EQ
Qualification
2/072017
71152B
Corrective Action
Documents
CR 1372336
Fatigue Rule Violation
2/28/2017
71152B
Corrective Action
Documents
CR 1378392
M-B ERCW Pump stopped due to rising bearing temps
01/18/2018
71152B
Corrective Action
Documents
CR 1380592
Equipment relocated during installation of plexi-glass
01/24/2018
71152B
Corrective Action
Documents
CR 1381347
NCV 2017008-01, Unjustified Qualified Life for Target
Rock PORVs
01/26/2018
71152B
Corrective Action
Documents
Documents
71152B    Corrective Action CR 1254937  NOER was not Generated for CR 1241933              01/26/2017
CR 1381348
NCV 2017008-02, Inadequate Qualification for Reactor
Lower Compartment Cooler Motors
01/26/2018
71152B
Corrective Action
Documents
Documents
71152B    Corrective Action CR 1255171  Gaps in Extent of Condition Review of QA Finding  01/26/2017
CR 1391505
Documents                    RCA 1155352
Deficiencies identified during mock 95001 inspection
71152B    Corrective Action CR 1255177  Trend in Site CAP Procedure Adherence to NPG-SPP-  01/26/2017
2/28/2018
Documents                    22.300
71152B
71152B    Corrective Action CR 1269767  A212 ABSCE Breach Resulting in Both Trains of      03/07/2017
Corrective Action
Documents                    ABGTS Inoperable for Both Units
71152B    Corrective Action CR 1290969  Snapshot Assessment - PD - SQN-PI-SSA-17-007 -    05/02/2017
Documents                    OE Coordinators
71152B     Corrective Action CR 1301718  Unit 1 TDAFW Suction Pressure Gauge Found          05/30/2017
Documents                    Isolated
71152B    Corrective Action CR 1303852  RP REP VANS                                        06/05/2017
Inspection Type              Designation Description or Title                                  Revision or
Procedure                                                                                      Date
Documents
Documents
71152B    Corrective Action CR 1305710  Procedure Change Request for 2-SI-SXV-003-219.S        06/10/2017
CR 1394115
OE - NRC Information Notice 2018-02
03/08/2018
71152B
Corrective Action
Documents
Documents
71152B    Corrective Action CR 1311223  QA ID: The Chemical Hygiene Plan was not reviewed      06/26/2017
CR 1403173
Documents                    during 2016 (SSA1707)
Boric acid valve leaking badly near BAT pump 1A
71152B    Corrective Action CR 1311501  QA ID: SSA1707: Inconsistent performance of            06/27/2017
04/09/2018
Documents                    surveillance procedure requirements
71152B
71152B    Corrective Action CR 1313355  Inadequate chain size used for temporary equipment    07/03/2017
Corrective Action
Documents                    seismic restraint
71152B    Corrective Action CR 1313866  OE-Green-WBN-NOER-17-014-Unplanned LCO 3.7.5          07/05/2017
Documents                    entry due to time delay relay failure
71152B     Corrective Action CR 1321168  Corrective Action for CR 1303852 did not resolve      07/25/2017
Documents                    condition identified
71152B    Corrective Action CR 1323549  QAID Improper use of N/A (SSA 1708)                    08/01/2017
Documents
Documents
71152B    Corrective Action CR 1323551  QA Records from ALARA not being transmitted to        08/01/2017
CR 1403747
Documents                    EDMS
SGI Records
71152B    Corrective Action CR 1323555  QAID Temporary Shielding forms not properly filled out 08/01/2017
04/09/2018
Documents                    (SSA 1708)
71152B
71152B     Corrective Action CR 1323558  QAID Recommendation on temporary shielding            08/01/2017
Corrective Action
Documents                    support (SSA 1708)
71152B    Corrective Action CR 1324371  Follow-up on CR 1324282 from SQN RP - RW Audit        08/03/2017
Documents
Documents
71152B    Corrective Action CR 1334122  NRC Regulatory Issue Summary (RIS) 2017-04             08/31/2017
CR 1403761
SGI Records
04/09/2018
71152B
Corrective Action
Documents
Documents
71152B     Corrective Action CR 1336290  Cable Tray Supports out of Tolerance                  09/07/2017
CR 1403896
Boric acid leak on Unit 2 emergency boration FT
instrument line
04/10/2018
71152B
Corrective Action
Documents
Documents
71152B     Corrective Action CR 1341686  Cable Tray Supports out of Tolerance                  09/25/2017
CR 1403944
SGI Records
04/10/2018
71152B
Corrective Action
Documents
CR 1403950
SGI Records
04/11/2018
71152B
Corrective Action
Documents
CR 1404549
1-LT-62-130 VCT Level Indication Failed Low
04/11/2018
71152B
Corrective Action
Documents
CR 1404590
LL BOP/NSSS DCS Loss of 62-130A
04/11/2018
71152B
Corrective Action
CR 1407364
U1R22 Outage WO Screening - FIN resources
04/20/2018
 
Inspection
Procedure
Type
Designation
Description or Title
Revision or
Date
Documents
Documents
71152B     Corrective Action CR 1343410  SGI records                                            09/29/2017
71152B
Corrective Action
Documents
Documents
71152B    Corrective Action CR 1364616  OE - Part 21 2017-52-00 Fisher Type 461 Valve Plug    12/04/2017
CR 1408522
Documents                    Machining
Issues found during performance of 1-SI-SXP-062-
71152B    Corrective Action CR 1366082  SQN DBA EQ 201700X                                    12/07/2017
203.0
Inspection Type              Designation Description or Title                                  Revision or
04/24/2018
Procedure                                                                                      Date
71152B
Corrective Action
Documents
Documents
71152B    Corrective Action CR 1366200  Unit 1 Lower Compartment Cooler Motor EQ              12/072017
CR 1408611
Documents                    Qualification
Troubleshoot CCP 1A Pump Vibration After U1R22
71152B    Corrective Action CR 1372336  Fatigue Rule Violation                                12/28/2017
Rebuild
04/24/2018
71152B
Corrective Action
Documents
Documents
71152B    Corrective Action CR 1378392  M-B ERCW Pump stopped due to rising bearing temps      01/18/2018
CR 1410388
Grout base plate under 1A CCP post U1R22
05/01/2018
71152B
Corrective Action
Documents
Documents
71152B    Corrective Action CR 1380592  Equipment relocated during installation of plexi-glass 01/24/2018
CR 1413732
Non-cited Violation (NCV) 05000327/328/2018001-01
05/11/2018
71152B
Corrective Action
Documents
Documents
71152B    Corrective Action CR 1381347  NCV 2017008-01, Unjustified Qualified Life for Target  01/26/2018
CR 1413734
Documents                    Rock PORVs
Non-cited Violation (NCV) 05000327/328/2018001-02
71152B    Corrective Action CR 1381348  NCV 2017008-02, Inadequate Qualification for Reactor  01/26/2018
05/11/2018
Documents                    Lower Compartment Cooler Motors
71152B
71152B    Corrective Action CR 1391505  Deficiencies identified during mock 95001 inspection  02/28/2018
Corrective Action
Documents
Documents
71152B    Corrective Action CR 1394115  OE - NRC Information Notice 2018-02                    03/08/2018
CR 1414850
NRC Identified Green NCV 390/2018410
05/15/2018
71152B
Corrective Action
Documents
Documents
71152B    Corrective Action CR 1403173  Boric acid valve leaking badly near BAT pump 1A        04/09/2018
CR 1416612
Vibration Point 8H in Alert Range
05/21/2018
71152B
Corrective Action
Documents
Documents
71152B    Corrective Action CR 1403747  SGI Records                                            04/09/2018
CR 1433166
Suspect B Train EGTS FS-65-44 Failed
07/22/2018
71152B
Corrective Action
Documents
Documents
71152B    Corrective Action CR 1403761  SGI Records                                            04/09/2018
CR 1436225
EGTS Licensee Event Report Required Information
08/02/2018
71152B
Corrective Action
Documents
Documents
71152B    Corrective Action CR 1403896  Boric acid leak on Unit 2 emergency boration FT        04/10/2018
CR 1443992
Documents                    instrument line
OE - Review NRC IN 18-09 Electrical Arc Flash
71152B    Corrective Action CR 1403944  SGI Records                                            04/10/2018
08/30/2018
71152B
Corrective Action
Documents
Documents
71152B    Corrective Action CR 1403950  SGI Records                                            04/11/2018
CR 1444099
Found leads lifted for an alarm on 1B diesel
08/31/2018
71152B
Corrective Action
Documents
Documents
71152B    Corrective Action CR 1404549  1-LT-62-130 VCT Level Indication Failed Low            04/11/2018
CR 1447183
OE - IN-18-10, Thermal Sleeve Flange Wear Leads to
Stuck Control Rod
09/13/2018
71152B
Corrective Action
Documents
Documents
71152B    Corrective Action CR 1404590  LL BOP/NSSS DCS Loss of 62-130A                        04/11/2018
CR 1449176
OE - NRC Regulatory Issue Summary 2018-04
09/20/2018
71152B
Corrective Action
Documents
Documents
71152B    Corrective Action CR 1407364  U1R22 Outage WO Screening - FIN resources              04/20/2018
CR 1463962
Inspection Type              Designation Description or Title                              Revision or
Inability to timely retrieve design records
Procedure                                                                                  Date
11/07/2018
71152B
Corrective Action
Documents
Documents
71152B    Corrective Action CR 1408522  Issues found during performance of 1-SI-SXP-062-  04/24/2018
CR 1471007
Documents                    203.0
EQ Binder SQN-SOL-002 baseline evaluation
71152B     Corrective Action CR 1408611  Troubleshoot CCP 1A Pump Vibration After U1R22    04/24/2018
11/29/2018
Documents                    Rebuild
71152B
71152B    Corrective Action CR 1410388  Grout base plate under 1A CCP post U1R22          05/01/2018
Corrective Action
Documents
Documents
71152B     Corrective Action CR 1413732  Non-cited Violation (NCV) 05000327/328/2018001-01  05/11/2018
CR 1476565
Minor Void Found in Emergency Boration Line Above
1-FT-62-137
2/18/2018
71152B
Corrective Action
CR 1477034
Gas void observed during performance of 1-SI-OPS-
2/19/2018  
 
Inspection
Procedure
Type
Designation
Description or Title
Revision or
Date
Documents
Documents
71152B     Corrective Action CR 1413734  Non-cited Violation (NCV) 05000327/328/2018001-02  05/11/2018
2-040.A U1 CCP piping vent
71152B
Corrective Action
Documents
Documents
71152B     Corrective Action CR 1414850  NRC Identified Green NCV 390/2018410              05/15/2018
CR 1482178
SQN Site Records List does not agree with NPG-SPP-
2.300 records (QA audit SSA1901)
01/14/2019
71152B
Corrective Action
Documents
Documents
71152B     Corrective Action CR 1416612  Vibration Point 8H in Alert Range                  05/21/2018
CR 1482468
QA ID: Department OE Coordinators have not
completed the required JFG (SSA1901)
01/15/2019
71152B
Corrective Action
Documents
Documents
71152B    Corrective Action CR 1433166  Suspect B Train EGTS FS-65-44 Failed              07/22/2018
CR 1482669
Biennial fleet wide self assessment of the OE program
not performed as required by NPG-SPP-22.500
01/15/2019
71152B
Corrective Action
Documents
Documents
71152B     Corrective Action CR 1436225  EGTS Licensee Event Report Required Information    08/02/2018
CR 1483225
Revision recommendation for NPG-SPP-22.300
01/17/2019
71152B
Corrective Action
Documents
Documents
71152B    Corrective Action CR 1443992  OE - Review NRC IN 18-09 Electrical Arc Flash      08/30/2018
CR 1483228
Revision recommendation for NPG-SPP-22.500
01/17/2019
71152B
Corrective Action
Documents
Documents
71152B     Corrective Action CR 1444099  Found leads lifted for an alarm on 1B diesel      08/31/2018
CR 1483291
Re-evaluate NPG-SPP-22.500 as quality related
01/17/2019
71152B
Corrective Action
Documents
Documents
71152B    Corrective Action CR 1447183  OE - IN-18-10, Thermal Sleeve Flange Wear Leads to 09/13/2018
CR 1485069
Documents                    Stuck Control Rod
2019 WBN PI&R Inspection - Issues with CR 1414850
71152B    Corrective Action CR 1449176  OE - NRC Regulatory Issue Summary 2018-04          09/20/2018
01/24/2019
71152B
Corrective Action
Documents
Documents
71152B     Corrective Action CR 1463962  Inability to timely retrieve design records        11/07/2018
CR 1488033
Non-cited Violation (NCV) 2018004-02
2/04/2019
71152B
Corrective Action
Documents
Documents
71152B     Corrective Action CR 1471007  EQ Binder SQN-SOL-002 baseline evaluation          11/29/2018
CR 1489420
Revise security procedure
2/08/2019
71152B
Corrective Action
Documents
Documents
71152B    Corrective Action CR 1476565  Minor Void Found in Emergency Boration Line Above  12/18/2018
CR 1490857
Documents                    1-FT-62-137
Rx Power Does not Respond Correctly to Manual
71152B    Corrective Action CR 1477034  Gas void observed during performance of 1-SI-OPS-  12/19/2018
Make-ups Calculated to Maintain Power Stable
Inspection Type              Designation Description or Title                                    Revision or
2/14/2019
Procedure                                                                                        Date
71152B
Documents                    062-040.A U1 CCP piping vent
Corrective Action
71152B    Corrective Action CR 1482178  SQN Site Records List does not agree with NPG-SPP-      01/14/2019
Documents                    22.300 records (QA audit SSA1901)
71152B    Corrective Action CR 1482468  QA ID: Department OE Coordinators have not              01/15/2019
Documents                    completed the required JFG (SSA1901)
71152B     Corrective Action CR 1482669  Biennial fleet wide self assessment of the OE program  01/15/2019
Documents                    not performed as required by NPG-SPP-22.500
71152B    Corrective Action CR 1483225  Revision recommendation for NPG-SPP-22.300              01/17/2019
Documents
Documents
71152B    Corrective Action CR 1483228  Revision recommendation for NPG-SPP-22.500              01/17/2019
CR 1490951
Evaluation of trend intrusion issues in manholes across
SQN
2/14/2019
71152B
Corrective Action
Documents
Documents
71152B    Corrective Action CR 1483291  Re-evaluate NPG-SPP-22.500 as quality related          01/17/2019
CR 1491065
Establish and sustain a culture of excellence in PU&A
in Chemistry
2/14/2019
71152B
Corrective Action
Documents
Documents
71152B    Corrective Action CR 1485069  2019 WBN PI&R Inspection - Issues with CR 1414850      01/24/2019
CR 1494149
OE - WBN Integrated Inspection Report Nov 2018
Findings
2/27/2019
71152B
Corrective Action
Documents
Documents
71152B    Corrective Action CR 1488033  Non-cited Violation (NCV) 2018004-02                    02/04/2019
CR 1498586
DCN 21287 contained an incorrect calculation for main
steam line radiation release rate
03/13/2019
71152B
Corrective Action
Documents
Documents
71152B    Corrective Action CR 1489420  Revise security procedure                              02/08/2019
CR 1500107
SQN-PI-FSA-19-002, PI&R Self Assessment
03/18/2019
71152B
Corrective Action
Documents
Documents
71152B    Corrective Action CR 1490857  Rx Power Does not Respond Correctly to Manual          02/14/2019
CR 1500629
Documents                    Make-ups Calculated to Maintain Power Stable
OE - IN-2019-01, Inadequate Evaluation of Temporary
71152B    Corrective Action CR 1490951  Evaluation of trend intrusion issues in manholes across 02/14/2019
Alterations
Documents                    SQN
03/20/2019
71152B    Corrective Action CR 1491065  Establish and sustain a culture of excellence in PU&A  02/14/2019
71152B
Documents                    in Chemistry
Corrective Action
71152B    Corrective Action CR 1494149  OE - WBN Integrated Inspection Report Nov 2018          02/27/2019
CR 1503036
Documents                    Findings
2017 SQN EQ DBA Inspection: Foxboro/Weed
71152B    Corrective Action CR 1498586  DCN 21287 contained an incorrect calculation for main  03/13/2019
03/28/2019  
Documents                    steam line radiation release rate
 
71152B    Corrective Action CR 1500107  SQN-PI-FSA-19-002, PI&R Self Assessment                03/18/2019
Inspection
Procedure
Type
Designation
Description or Title
Revision or
Date
Documents
Documents
71152B    Corrective Action CR 1500629  OE - IN-2019-01, Inadequate Evaluation of Temporary    03/20/2019
Transmitter heat rise issue, SLD.
Documents                    Alterations
71152B
71152B    Corrective Action CR 1503036  2017 SQN EQ DBA Inspection: Foxboro/Weed                03/28/2019
Corrective Action
Inspection Type              Designation Description or Title                                  Revision or
Procedure                                                                                      Date
Documents                    Transmitter heat rise issue, SLD.
71152B     Corrective Action CR 1503045  2017 SQN EQ DBA Inspection: ASCO valves potential    03/28/2019
Documents                    performance deficiencies, SLD
71152B    Corrective Action CR 1503045  2017 SQN EQ DBA Inspection - ASCO valves potential    03/28/2019
Documents                    performance deficiencies
71152B    Corrective Action CR 1506308  Non-cited Violation (NCV) 2018412-01                  04/09/2019
Documents
Documents
71152B    Corrective Action CR 1506325  Replace U1 LCC Fan Motors during U1R24                04/09/2019
CR 1503045
2017 SQN EQ DBA Inspection: ASCO valves potential
performance deficiencies, SLD
03/28/2019
71152B
Corrective Action
Documents
Documents
71152B     Corrective Action CR 1506831 Review Unusual Event at Brunswick Unit 1 which       04/10/2019
CR 1503045
Documents                    required a shutdown
2017 SQN EQ DBA Inspection - ASCO valves potential
71152B    Corrective Action CR 1509174 Respond to NRC RIS 2019-02, Preparation and           04/18/2019
performance deficiencies
Documents                    Scheduling of Operator Licensing Examinations
03/28/2019
71152B     Corrective Action CR 1510339 SQN-PI-FSA-10-002 - Objective 7 - Appendix R         04/23/2019
71152B
Documents                    Triennial Inspection CR 1276596 has not been
Corrective Action
Documents
CR 1506308
Non-cited Violation (NCV) 2018412-01
04/09/2019
71152B
Corrective Action
Documents
CR 1506325
Replace U1 LCC Fan Motors during U1R24
04/09/2019
71152B
Corrective Action
Documents
CR 1506831
Review Unusual Event at Brunswick Unit 1 which
required a shutdown
04/10/2019
71152B
Corrective Action
Documents
CR 1509174
Respond to NRC RIS 2019-02, Preparation and
Scheduling of Operator Licensing Examinations
04/18/2019
71152B
Corrective Action
Documents
CR 1510339
SQN-PI-FSA-10-002 - Objective 7 - Appendix R
Triennial Inspection CR 1276596 has not been
resolved timely
resolved timely
71152B    Corrective Action CR 1510464  CR 1485069 did not document department manager        04/23/2019
04/23/2019
Documents                    approval
71152B
71152B    Corrective Action CR 1510873  SQN-PI-FSA-19-002 - Objective 7 - Deficiencies noted  04/24/2019
Corrective Action
Documents                    in CRs 1403944, 1441458, and 1403761
71152B    Corrective Action CR 1510985  SQN-PI-FSA-!(-002 - Objective 7 PD - A Review of      04/24/2019
Documents                    NCV 2017008-01
71152B    Corrective Action CR 1511003  SQN-PI-FSA-19-002 - Objective 7 PD - A Review of      04/24/2019
Documents                    NCV 2017008-02
71152B     Corrective Action CR 1511249  SQN-PI-FSA-19-002 Objective 7 PD (1500107-033)        04/25/2019
Documents                    LER-2018-001-00
71152B    Corrective Action CR 1512747  Non-cited Violation (NCV) 05000327/328/2019010-01    05/01/2019
Documents
Documents
71152B    Corrective Action CR 1514352  QA elevation on protected equipment                  05/06/2019
CR 1510464
CR 1485069 did not document department manager
approval
04/23/2019
71152B
Corrective Action
Documents
Documents
71152B    Corrective Action CR 1516824  NCV 2019-02, Failure to account for heat rise in      05/15/2019
CR 1510873
Documents                    Foxboro/Weed instruments
SQN-PI-FSA-19-002 - Objective 7 - Deficiencies noted
71152B    Corrective Action CR 1519228  Gas/water Flow Noted During Cold Leg Injection Piping 05/23/2019
in CRs 1403944, 1441458, and 1403761
Documents                    Vent
04/24/2019
Inspection Type              Designation Description or Title                                Revision or
71152B
Procedure                                                                                    Date
Corrective Action
71152B     Corrective Action CR 1525798  OE - Issues with OE Reviews in Accordance with      06/18/2019
Documents                    NPG-SPP-22.600
71152B    Corrective Action CR 655554  Loop 4 TDAFW LCV failed stroke time                12/12/2012
Documents
Documents
71152B    Corrective Action CR 660015  OE review of WBN-NOER-12-079                        12/21/2012
CR 1510985
SQN-PI-FSA-!(-002 - Objective 7 PD - A Review of
NCV 2017008-01
04/24/2019
71152B
Corrective Action
Documents
Documents
71152B    Corrective Action CR 663698  Review of WBN-NOER-12-106 AFW valve stroke time    01/04/2013
CR 1511003
SQN-PI-FSA-19-002 - Objective 7 PD - A Review of
NCV 2017008-02
04/24/2019
71152B
Corrective Action
Documents
Documents
71152B     Corrective Action CR 740635  SGTR accident analysis issue related to maintenance 06/14/2013
CR 1511249
SQN-PI-FSA-19-002 Objective 7 PD (1500107-033)
LER-2018-001-00
04/25/2019
71152B
Corrective Action
Documents
Documents
71152B    Corrective Action CR 750649  SQN review of Byron U2 scram from loss of main      07/09/2013
CR 1512747
Documents                    generator stator cooling
Non-cited Violation (NCV) 05000327/328/2019010-01
71152B    Corrective Action CR 751276  SQN review of Vogtle U2 manual reactor scram due to 07/10/2013
05/01/2019
Documents                    high RCP seal leak off
71152B
71152B     Corrective Action CR 791573  SQN review of Davis-Besse scram from RCP motor      10/10/2013
Corrective Action
Documents                    faulty electrical connections
71152B    Corrective Action CR 915358  Unit 2 main turbine high vibration                  07/30/2014
Documents
Documents
71152B    Corrective Action CR 959976  Aging management review for ground water in        11/24/2014
CR 1514352
Documents                    distribution board
QA elevation on protected equipment
71152B    Corrective Action CR 965728  Procedure swap performed with step marked N/A that  12/10/2014
05/06/2019
Documents                    resulted in configuration control issue
71152B
71152B    Corrective Action CR 973446  2B MDAFW system check valve backleakage            01/05/2015
Corrective Action
Documents
Documents
71152B     Corrective Action CR 981733  Low oil on 2A MDAFWP inboard pump bearing          01/27/2015
CR 1516824
NCV 2019-02, Failure to account for heat rise in
Foxboro/Weed instruments
05/15/2019
71152B
Corrective Action
Documents
Documents
71152B     Corrective Action CR 1522084  Broken UNID tag                                    06/04/2019
CR 1519228
Gas/water Flow Noted During Cold Leg Injection Piping
Vent
05/23/2019
 
Inspection
Procedure
Type
Designation
Description or Title
Revision or
Date
71152B
Corrective Action
Documents
CR 1525798
OE - Issues with OE Reviews in Accordance with
NPG-SPP-22.600
06/18/2019
71152B
Corrective Action
Documents
CR 655554
Loop 4 TDAFW LCV failed stroke time
2/12/2012
71152B
Corrective Action
Documents
CR 660015
OE review of WBN-NOER-12-079
2/21/2012
71152B
Corrective Action
Documents
CR 663698
Review of WBN-NOER-12-106 AFW valve stroke time
01/04/2013
71152B
Corrective Action
Documents
CR 740635
SGTR accident analysis issue related to maintenance
06/14/2013
71152B
Corrective Action
Documents
CR 750649
SQN review of Byron U2 scram from loss of main
generator stator cooling
07/09/2013
71152B
Corrective Action
Documents
CR 751276
SQN review of Vogtle U2 manual reactor scram due to
high RCP seal leak off
07/10/2013
71152B
Corrective Action
Documents
CR 791573
SQN review of Davis-Besse scram from RCP motor
faulty electrical connections
10/10/2013
71152B
Corrective Action
Documents
CR 915358
Unit 2 main turbine high vibration
07/30/2014
71152B
Corrective Action
Documents
CR 959976
Aging management review for ground water in
distribution board
11/24/2014
71152B
Corrective Action
Documents
CR 965728
Procedure swap performed with step marked N/A that
resulted in configuration control issue
2/10/2014
71152B
Corrective Action
Documents
CR 973446
2B MDAFW system check valve backleakage
01/05/2015
71152B
Corrective Action
Documents
CR 981733
Low oil on 2A MDAFWP inboard pump bearing
01/27/2015
71152B
Corrective Action
Documents
Documents
Resulting from
Resulting from
Inspection
Inspection
71152B    Corrective Action CR 1522525  Procedure NPG-SPP-22.300 change request            06/05/2019
CR 1522084
Broken UNID tag
06/04/2019
71152B
Corrective Action
Documents
Documents
Resulting from
Resulting from
Inspection
Inspection
Inspection Type             Designation Description or Title                                 Revision or
CR 1522525
Procedure                                                                                    Date
Procedure NPG-SPP-22.300 change request
71152B     Corrective Action CR 1525710  Individual missed 2018 SCWE Training - CO issue      06/18/2019
06/05/2019
 
Inspection
Procedure
Type
Designation
Description or Title
Revision or
Date
71152B
Corrective Action
Documents
Documents
Resulting from
Resulting from
Inspection
Inspection
71152B    Corrective Action CR 1525830  NRC ID - ERB package documentation error - CO       06/18/2019
CR 1525710
Documents                     issue
Individual missed 2018 SCWE Training - CO issue
06/18/2019
71152B
Corrective Action
Documents
Resulting from
Resulting from
Inspection
Inspection
71152B    Corrective Action CR 1525832  NPG-SPP-03.9 wording of Significant Gap Analysis not 06/18/2019
CR 1525830
Documents                     matching NPG-SPP-22.300
NRC ID - ERB package documentation error - CO
issue
06/18/2019
71152B
Corrective Action
Documents
Resulting from
Resulting from
Inspection
Inspection
71152B    Corrective Action CR 1525869  NOER-SQN-17-003 has incorrect event date            06/18/2019
CR 1525832
NPG-SPP-03.9 wording of Significant Gap Analysis not
matching NPG-SPP-22.300
06/18/2019
71152B
Corrective Action
Documents
Documents
Resulting from
Resulting from
Inspection
Inspection
71152B    Corrective Action CR 1526184  Extension request reason insufficient                06/19/2019
CR 1525869
NOER-SQN-17-003 has incorrect event date
06/18/2019
71152B
Corrective Action
Documents
Documents
Resulting from
Resulting from
Inspection
Inspection
71152B    Corrective Action CR 1526337  Incorrect Maximo attachments                        06/20/2019
CR 1526184
Extension request reason insufficient
06/19/2019
71152B
Corrective Action
Documents
Documents
Resulting from
Resulting from
Inspection
Inspection
71152B    Corrective Action CR 1526428  Inadequate response to CRs                          06/20/2019
CR 1526337
Incorrect Maximo attachments
06/20/2019
71152B
Corrective Action
Documents
Documents
Resulting from
Resulting from
Inspection
Inspection
71152B     Engineering       DCN 23813   Replace Steam Generator Blowdown Containment         Revision 1
CR 1526428
Changes                      Isolation Sample Valves
Inadequate response to CRs
71152B     Miscellaneous                 U2 Function 043-E (a)(1) plan                       Revision 2
06/20/2019
71152B     Miscellaneous                 Quality Assurance Master Audit Schedule 2019-2020   08/29/2017
71152B
71152B     Miscellaneous                 Browns Ferry Nuclear Plant, Sequoyah Nuclear Plant, 05/09/2008
Engineering
Changes
DCN 23813
Replace Steam Generator Blowdown Containment
Isolation Sample Valves
Revision 1
71152B
Miscellaneous
U2 Function 043-E (a)(1) plan
Revision 2
71152B
Miscellaneous
Quality Assurance Master Audit Schedule 2019-2020
08/29/2017
71152B
Miscellaneous
Browns Ferry Nuclear Plant, Sequoyah Nuclear Plant,
and Watts Bar Nuclear Plant Initial Response to NRC
and Watts Bar Nuclear Plant Initial Response to NRC
Inspection Type         Designation       Description or Title                                 Revision or
05/09/2008
Procedure                                                                                        Date
 
Inspection
Procedure
Type
Designation
Description or Title
Revision or
Date
Generic Letter 2008-01
Generic Letter 2008-01
71152B     Miscellaneous                   Sequoyah Nuclear Plant - Closeout of Generic Letter 04/22/2011
71152B
Miscellaneous
Sequoyah Nuclear Plant - Closeout of Generic Letter
2008-01
2008-01
71152B     Miscellaneous                   Operations Standing Order List                       06/05/2019
04/22/2011
71152B     Miscellaneous                   Chemical and Volume Control System (CVCS) Health     1st Quarter
71152B
Report Scorecard                                    2019
Miscellaneous
71152B     Miscellaneous                   SQN Maintenance Rule List - SSCs in (a)(1) Status
Operations Standing Order List
06/05/2019
71152B
Miscellaneous
Chemical and Volume Control System (CVCS) Health
Report Scorecard
1st Quarter
2019
71152B
Miscellaneous
SQN Maintenance Rule List - SSCs in (a)(1) Status
since June 2017
since June 2017
71152B     Miscellaneous                   Unit 1 MCR Deficiencies List                         06/05/2019
71152B
71152B     Miscellaneous                   Unit 2 MCR Deficiencies List                         06/05/2019
Miscellaneous
71152B     Miscellaneous                   System #333 Health Report Screenshot
Unit 1 MCR Deficiencies List
71152B     Miscellaneous CDE 2855           2-FSV-43-61 PAM indication inoperable for 30 days   08/28/2015
06/05/2019
71152B     Miscellaneous CDE 2884           2-FSV-43-61 no light indication in main control room 01/04/2016
71152B
71152B     Miscellaneous CDE 2886           2-FSV-43-55 Failed 2-SI-SXV-043-204.0               12/09/2015
Miscellaneous
71152B     Miscellaneous CDE 2903           2-FSV-43-61 PAM instrument had dual light position   05/10/2016
Unit 2 MCR Deficiencies List
06/05/2019
71152B
Miscellaneous
System #333 Health Report Screenshot
71152B
Miscellaneous
CDE 2855
2-FSV-43-61 PAM indication inoperable for 30 days
08/28/2015
71152B
Miscellaneous
CDE 2884
2-FSV-43-61 no light indication in main control room
01/04/2016
71152B
Miscellaneous
CDE 2886
2-FSV-43-55 Failed 2-SI-SXV-043-204.0
2/09/2015
71152B
Miscellaneous
CDE 2903
2-FSV-43-61 PAM instrument had dual light position
indications
indications
71152B     Miscellaneous MRC               Management Review Committee Package                 06/06/2019
05/10/2016
71152B     Miscellaneous PSC               Plant Screening Committee Package                   06/05/2019
71152B
71152B     Miscellaneous QA-SQ-18-006       Sequoyah Nuclear Plant - Quality Assurance Site     03/14/2018
Miscellaneous
MRC
Management Review Committee Package
06/06/2019
71152B
Miscellaneous
PSC
Plant Screening Committee Package
06/05/2019
71152B
Miscellaneous
QA-SQ-18-006
Sequoyah Nuclear Plant - Quality Assurance Site
Report
Report
71152B     Miscellaneous QA-SQ-19-002       Sequoyah Nuclear Plant - Quality Assurance Site     02/07/2019
03/14/2018
71152B
Miscellaneous
QA-SQ-19-002
Sequoyah Nuclear Plant - Quality Assurance Site
Report
Report
71152B     Miscellaneous QA-SQ-19-004       Sequoyah Nuclear Plant - Quality Assurance Site     03/11/2019
2/07/2019
71152B
Miscellaneous
QA-SQ-19-004
Sequoyah Nuclear Plant - Quality Assurance Site
Report
Report
71152B     Miscellaneous QA-SQ-19-006       Sequoyah Nuclear Plant - Quality Assurance Site     04/08/2019
03/11/2019
71152B
Miscellaneous
QA-SQ-19-006
Sequoyah Nuclear Plant - Quality Assurance Site
Report
Report
71152B     Miscellaneous QA-SQ-19-008       Sequoyah Nuclear Plant - Quality Assurance Site     05/09/2019
04/08/2019
71152B
Miscellaneous
QA-SQ-19-008
Sequoyah Nuclear Plant - Quality Assurance Site
Report
Report
71152B     Miscellaneous SQN-DC-V-13.9.8   Sequoyah Nuclear Plant - Auxiliary Feedwater System, Revision 29
05/09/2019
71152B
Miscellaneous
SQN-DC-V-13.9.8
Sequoyah Nuclear Plant - Auxiliary Feedwater System,
Design Criteria Document
Design Criteria Document
71152B     Miscellaneous SQN-DC-V-27.2     Sequoyah Nuclear Plant - Chemical and Volume         Revision 35
Revision 29
71152B
Miscellaneous
SQN-DC-V-27.2
Sequoyah Nuclear Plant - Chemical and Volume
Control System, Design Criteria
Control System, Design Criteria
71152B     Miscellaneous UFSAR Chapter 13.9 License Renewal Program                             Revision 26
Revision 35
71152B     Procedures   0-MI-MRR-003-461.0 Disassembly, Inspection, and Reassembly of the       Revision 26
71152B
Inspection Type       Designation       Description or Title                                 Revision or
Miscellaneous
Procedure                                                                                      Date
UFSAR Chapter 13.9
License Renewal Program
Revision 26
71152B
Procedures
0-MI-MRR-003-461.0
Disassembly, Inspection, and Reassembly of the
Revision 26  
 
Inspection
Procedure
Type
Designation
Description or Title
Revision or
Date
Auxiliary Feedwater Pump Turbine
Auxiliary Feedwater Pump Turbine
71152B     Procedures 1-SI-IFT-068-067.4 Functional Test of Delta T/TAVG Channel IV Rack 13   Revision 28
71152B
Procedures
1-SI-IFT-068-067.4
Functional Test of Delta T/TAVG Channel IV Rack 13
Loop 1-T-68-67 (T-441/442)
Loop 1-T-68-67 (T-441/442)
71152B     Procedures 1-SI-OPS-062-040.A Centrifugal Charging Pump 1A-A Casing, Suction, and Revision 42
Revision 28
71152B
Procedures
1-SI-OPS-062-040.A
Centrifugal Charging Pump 1A-A Casing, Suction, and
Discharge Piping Venting
Discharge Piping Venting
71152B     Procedures NPG-SPP-03.4       Maintenance Rule Performance Indicator Monitoring,   Revision 3
Revision 42
71152B
Procedures
NPG-SPP-03.4
Maintenance Rule Performance Indicator Monitoring,
Trending and Reporting - 10CFR50.65
Trending and Reporting - 10CFR50.65
71152B     Procedures NPG-SPP-07.1.4     Work Management Prioritization - Online             Revision 9
Revision 3
71152B     Procedures NPG-SPP-07.6       NPG Work Management Planning Procedure               Revision 15
71152B
71152B     Procedures NPG-SPP-07.6       NPG Work Management Planning Procedure               Revision 16
Procedures
71152B     Procedures NPG-SPP-22.300     Corrective Action Program                           Revision 14
NPG-SPP-07.1.4
71152B     Procedures NPG-SPP-22.300     Corrective Action Program                           Revision 15
Work Management Prioritization - Online
71152B     Procedures NPG-SPP-22.300     Corrective Action Program                           Revision 12
Revision 9
71152B     Procedures NPG-SPP-22.300     Corrective Action Program                           Revision 10
71152B
71152B     Procedures NPG-SPP-22.500     Operating Experience Program                         Revision 7
Procedures
71152B     Procedures NPG-SPP-22.600     Issue Resolution                                     Revision 5
NPG-SPP-07.6
71152B     Procedures OPDP-1             Conduct of Operations                               Revision 43
NPG Work Management Planning Procedure
71152B     Procedures OPDP-11           Operational Decision-Making Issue Evaluation Process Revision 6
Revision 15
71152B     Procedures OPDP-4             Annunciator Disablement                             Revision 7
71152B
71152B     Self-       SSA1701           Site Audit Report, Corrective Action Program,       02/22/2017
Procedures
Assessments                    Sequoyah Nuclear Plant (SQN), January 23-27, 2017
NPG-SPP-07.6
71152B     Self-       SSA1707           Site Audit Report, Chemistry, Effluent, and         07/17/2017
NPG Work Management Planning Procedure
Assessments                    Environmental Monitoring, Sequoyah Nuclear Plant
Revision 16
                                          (SQN), June 19-30, 2017
71152B
71152B     Self-       SSA1708           Site Audit Report, Radiation Protection, Radwaste,   08/10/2017
Procedures
Assessments                    Sequoyah Nuclear Plant (SQN), July 24-August 2,
NPG-SPP-22.300
Corrective Action Program
Revision 14
71152B
Procedures
NPG-SPP-22.300
Corrective Action Program
Revision 15
71152B
Procedures
NPG-SPP-22.300
Corrective Action Program
Revision 12
71152B
Procedures
NPG-SPP-22.300
Corrective Action Program
Revision 10
71152B
Procedures
NPG-SPP-22.500
Operating Experience Program
Revision 7
71152B
Procedures
NPG-SPP-22.600
Issue Resolution
Revision 5
71152B
Procedures
OPDP-1
Conduct of Operations
Revision 43
71152B
Procedures
OPDP-11
Operational Decision-Making Issue Evaluation Process
Revision 6
71152B
Procedures
OPDP-4
Annunciator Disablement
Revision 7
71152B
Self-
Assessments
SSA1701
Site Audit Report, Corrective Action Program,
Sequoyah Nuclear Plant (SQN), January 23-27, 2017
2/22/2017
71152B
Self-
Assessments
SSA1707
Site Audit Report, Chemistry, Effluent, and
Environmental Monitoring, Sequoyah Nuclear Plant  
(SQN), June 19-30, 2017
07/17/2017
71152B
Self-
Assessments
SSA1708
Site Audit Report, Radiation Protection, Radwaste,
Sequoyah Nuclear Plant (SQN), July 24-August 2,
2017
2017
71152B     Self-       SSA1804           Site Audit Report, Maintenance, Sequoyah Nuclear     04/20/2018
08/10/2017
Assessments                    Station (SQN), March 26-April 6, 2018
71152B
71152B     Self-       SSA1901           Corrective Action, Chattanooga Office Complex (COC), 01/30/2019
Self-
Assessments                    Browns Ferry (BFN), Sequoyah (SQN) and Watts Bar
Assessments
                                          (WBN) Nuclear Plants, January 14-18, 2019
SSA1804
71152B     Work Orders 113086647         Replace Unit 2 PORVs
Site Audit Report, Maintenance, Sequoyah Nuclear
71152B     Work Orders 113574449         Replace current control unit for 2-FSV-043-0055-B
Station (SQN), March 26-April 6, 2018
Inspection Type             Designation Description or Title                                 Revision or
04/20/2018
Procedure                                                                                      Date
71152B
71152B     Work Orders       115152446   Replace Unit 2 PORVs
Self-
71152B     Work Orders       117485917   Steam Generator Blowdown #3 Isolation Valve has no
Assessments
SSA1901
Corrective Action, Chattanooga Office Complex (COC),
Browns Ferry (BFN), Sequoyah (SQN) and Watts Bar  
(WBN) Nuclear Plants, January 14-18, 2019
01/30/2019
71152B
Work Orders
113086647
Replace Unit 2 PORVs
71152B
Work Orders
113574449
Replace current control unit for 2-FSV-043-0055-B  
 
Inspection
Procedure
Type
Designation
Description or Title
Revision or
Date
71152B
Work Orders
115152446
Replace Unit 2 PORVs
71152B
Work Orders
117485917
Steam Generator Blowdown #3 Isolation Valve has no
Light Indication in MCR
Light Indication in MCR
71152B     Work Orders       117715470   Calibrate TDAFWP inlet pressure indicator
71152B
71152B     Work Orders       117733991   Perform additional groundwater in-leakage repairs in
Work Orders
117715470
Calibrate TDAFWP inlet pressure indicator
71152B
Work Orders
117733991
Perform additional groundwater in-leakage repairs in
various yard areas
various yard areas
71152B     Work Orders       117910082   Inspect and clean 250 VDC battery board #2
71152B
71152B     Work Orders       118800008   Replace EGTS Train B electronic circuit board
Work Orders
71152B     Work Orders       118878733   DCN 23638 Stage 8 outage cable terminations and
117910082
Inspect and clean 250 VDC battery board #2
71152B
Work Orders
118800008
Replace EGTS Train B electronic circuit board
71152B
Work Orders
118878733
DCN 23638 Stage 8 outage cable terminations and
modifications
modifications
71152B     Work Orders       118888040   Inadequate chain size used for temporary equipment
71152B
Work Orders
118888040
Inadequate chain size used for temporary equipment
seismic restraint
seismic restraint
71152B     Work Orders       118946474   Replace 1-RLY-62-108/CPBY-1A due to Part 21 issue
71152B
71152B     Work Orders       119111157   Perform groundwater in-leakage repairs in various
Work Orders
118946474
Replace 1-RLY-62-108/CPBY-1A due to Part 21 issue
71152B
Work Orders
119111157
Perform groundwater in-leakage repairs in various
areas for the Auxiliary Building
areas for the Auxiliary Building
71152B     Work Orders       119444328   Rewind or replace 1B-B LCC fan motor to resolve
71152B
Work Orders
119444328
Rewind or replace 1B-B LCC fan motor to resolve
NCV, CR 1381348
NCV, CR 1381348
71152B     Work Orders       119444348   Rewind or replace 1C-A LCC fan motor to resolve
71152B
Work Orders
119444348
Rewind or replace 1C-A LCC fan motor to resolve
NCV, CR 1381348
NCV, CR 1381348
71152B     Work Orders       119444352   Rewind or replace 1D-B LCC fan motor to resolve
71152B
Work Orders
119444352
Rewind or replace 1D-B LCC fan motor to resolve
NCV, CR 1381348
NCV, CR 1381348
71152B     Work Orders       119448481   Rewind or replace 1A-A LCC fan motor to resolve
71152B
Work Orders
119448481
Rewind or replace 1A-A LCC fan motor to resolve
NCV, CR 1381348
NCV, CR 1381348
71152B     Work Orders       119529017   1-LT-62-130 VCT level indication has failed low
71152B
71152B     Work Orders       119568924   1A CCP grout base plate
Work Orders
71152B     Work Orders       119855356   Implement DCN 22643 Stage 6 to replace U1 PORV
119529017
1-LT-62-130 VCT level indication has failed low
71152B
Work Orders
119568924
1A CCP grout base plate
71152B
Work Orders
119855356
Implement DCN 22643 Stage 6 to replace U1 PORV
334-B
334-B
71152B     Work Orders       119855374   Implement DCN 22643 Stage 5 to replace U1 PORV
71152B
Work Orders
119855374
Implement DCN 22643 Stage 5 to replace U1 PORV
340A-A
340A-A
71152B     Work Orders       120398985  Replace U1 1A-A LCC Fan Motors during U1R24
71152B
71152B     Work Orders       120398986  Replace U1 1D-B LCC Fan Motor during U1R24
Work Orders
71152B     Work Orders       120398987  Replace U1 1C-A LCC Fan Motor during U1R24
20398985
71152B     Work Orders       120398988  Replace U1 1B-B LCC Fan Motor during U1R24
Replace U1 1A-A LCC Fan Motors during U1R24
2702     Corrective Action 1322419    Action Implementation Tracking for Confirmatory Order
71152B
Inspection Type             Designation Description or Title                                 Revision or
Work Orders
Procedure                                                                                      Date
20398986
Documents                     EA-17-022
Replace U1 1D-B LCC Fan Motor during U1R24
2702     Corrective Action 1404011     Sequoyahs response to the Oak Ridge Associated
71152B
CONF      Documents                    Universities nuclear safety culture assessment report
Work Orders
2702     Corrective Action 1416534     Track Corporate's response to NSC assessment.
20398987
CONF       Documents
Replace U1 1C-A LCC Fan Motor during U1R24
2702      Corrective Action 1448122     OE.01.NUC.01-Sustain TVA Nuclear Work
71152B
CONF      Documents                    Environment
Work Orders
2702     Corrective Action 1451197-003 SCWE Mitigation Plan follow up actions for corporate
20398988
CONF      Documents                    ERB case numbers CORP-2019-010, 011, 012, 013
Replace U1 1B-B LCC Fan Motor during U1R24
2702
Corrective Action
22419
Action Implementation Tracking for Confirmatory Order  
 
Inspection
Procedure
Type
Designation
Description or Title
Revision or
Date
Documents
EA-17-022
2702
CONF
Corrective Action
Documents
1404011
Sequoyahs response to the Oak Ridge Associated
Universities nuclear safety culture assessment report
2702
CONF
Corrective Action
Documents
1416534
Track Corporate's response to NSC assessment.
2702
CONF
Corrective Action
Documents
1448122
OE.01.NUC.01-Sustain TVA Nuclear Work
Environment
2702
CONF
Corrective Action
Documents
1451197-003
SCWE Mitigation Plan follow up actions for corporate
ERB case numbers CORP-2019-010, 011, 012, 013
and 014
and 014
2702     Corrective Action 1477964     LMS Curriculum NPG-TVA-400152, SCWE EA 17-022
2702
CONF      Documents                    incorrect due dates
CONF
2702     Corrective Action 1478023     LMS Curriculum NPG-TVA-400152, SCWE EA 17-022
Corrective Action
CONF      Documents                    is calculating incorrect due date
Documents
2702     Corrective Action 1484364     Action Tracking for SQN SCWE Refresher Training
1477964
CONF       Documents
LMS Curriculum NPG-TVA-400152, SCWE EA 17-022
2702      Corrective Action 1492600     Safety Culture
incorrect due dates
CONF       Documents
2702
2702      Corrective Action 1497144     EA-17-022, Section V.1.b.3 90-day SCWE training
CONF
CONF      Documents                    requirement not met
Corrective Action
2702     Corrective Action 1525830    Discrepancy in ERB 2018-031 TVA Forms 41647 (item
Documents
CONF      Documents                     # 3) and 41651 (item # 1)
1478023
LMS Curriculum NPG-TVA-400152, SCWE EA 17-022
is calculating incorrect due date
2702
CONF
Corrective Action
Documents
1484364
Action Tracking for SQN SCWE Refresher Training
2702
CONF
Corrective Action
Documents
1492600
Safety Culture
2702
CONF
Corrective Action
Documents
1497144
EA-17-022, Section V.1.b.3 90-day SCWE training
requirement not met
2702
CONF
Corrective Action
Documents
Resulting from
Resulting from
Inspection
Inspection
2702     Corrective Action 1526768    ECP Benchmarking not documented per NPG-SPP-
25830
CONF      Documents                     22.102
Discrepancy in ERB 2018-031 TVA Forms 41647 (item
# 3) and 41651 (item # 1)
2702
CONF
Corrective Action
Documents
Resulting from
Resulting from
Inspection
Inspection
2702     Miscellaneous                 Sequoyah Nuclear Plant Nuclear Safety Culture         April 2018
26768
CONF                                    Evaluation, prepared by Oak Ridge Associated
ECP Benchmarking not documented per NPG-SPP-
2.102
2702
CONF
Miscellaneous
Sequoyah Nuclear Plant Nuclear Safety Culture
Evaluation, prepared by Oak Ridge Associated
Universities
Universities
2702     Procedures                   Conduct of Operations Employee Concerns               Revision 7
April 2018
2702
CONF
Procedures
Conduct of Operations Employee Concerns
Revision 7
2702
Procedures
1193005
Business Plan Initiative OE.01.Nuc.01 (Improve TVA
 
Inspection
Procedure
Type
Designation
Description or Title
Revision or
Date
CONF
Nuclear Work Environment)
2702
CONF
Procedures
ECP-1
Employee Concerns Staff Desktop Instruction 1 ECP
Administration
Revision 0
2702
CONF
Procedures
NPG-SPP-01.7
Nuclear Safety Culture
Revision 5
2702
CONF
Procedures
NPG-SPP-01.7.1
Employee Concerns Program
Revision 3
2702
CONF
CONF
2702      Procedures        1193005    Business Plan Initiative OE.01.Nuc.01 (Improve TVA
Procedures
Inspection Type      Designation    Description or Title                              Revision or
NPG-SPP-01.7.2
Procedure                                                                              Date
Nuclear Safety Culture Monitoring
CONF                                Nuclear Work Environment)
Revision 13
2702      Procedures ECP-1          Employee Concerns Staff Desktop Instruction 1 ECP Revision 0
2702
CONF                                Administration
2702      Procedures NPG-SPP-01.7   Nuclear Safety Culture                           Revision 5
CONF
CONF
2702      Procedures NPG-SPP-01.7.1 Employee Concerns Program                        Revision 3
Procedures
NPG-SPP-01.7.3
Conduct of Nuclear Safety Culture Assessments and
Organizational Effectiveness Surveys
Revision 4
2702
CONF
CONF
2702      Procedures NPG-SPP-01.7.2 Nuclear Safety Culture Monitoring                Revision 13
Procedures
NPG-SPP-01.7.4
Adverse Employment Action and Executive Review
Board
Revision 1
2702
CONF
CONF
2702      Procedures NPG-SPP-01.7.3 Conduct of Nuclear Safety Culture Assessments and Revision 4
Procedures
CONF                                Organizational Effectiveness Surveys
NPG-SPP-01.7.4
2702      Procedures NPG-SPP-01.7.4 Adverse Employment Action and Executive Review   Revision 1
Adverse Employment Action and Executive Review
CONF                                Board
Board
2702      Procedures NPG-SPP-01.7.4 Adverse Employment Action and Executive Review    Revision 3
Revision 3
CONF                                Board
2702
2702     Procedures TVA-SPP-22.100 Change Management                                Revision 0
CONF
CONF
23
Procedures
TVA-SPP-22.100
Change Management
Revision 0
}}
}}

Latest revision as of 01:04, 5 January 2025

Biennial Problem Identification and Resolution Inspection Report 05000327/2019011 and 05000328/2019011
ML19204A190
Person / Time
Site: Sequoyah  Tennessee Valley Authority icon.png
Issue date: 07/23/2019
From: Omar Lopez-Santiago
Division Reactor Projects II
To: James Shea
Tennessee Valley Authority
Reeder D
References
IR 2019011
Download: ML19204A190 (26)


Text

July 23, 2019

SUBJECT:

SEQUOYAH NUCLEAR PLANT - BIENNIAL PROBLEM IDENTIFICATION AND RESOLUTION INSPECTION REPORT 05000327/2019011 AND 05000328/2019011

Dear Mr. Shea:

On June 27, 2019, the U.S. Nuclear Regulatory Commission (NRC) completed a problem identification and resolution inspection at your Sequoyah Nuclear Plant, Units 1 and 2. On June 20 and 27, 2019, the inspectors discussed the results of this inspection with Mr. Matthew Rasmussen and other members of your staff. The results of this inspection are documented in the enclosed report.

As stated in your 2017 Annual Assessment Letter (ML18059A143), dated February 28, 2018, the International Atomic Energy Association (IAEA) Operational Safety Review Team (OSART)

inspection completed at your facility in 2017, entitled you to a one-time credit to the baseline inspection of the Reactor Oversight Process (ROP). As such, NRC inspection hours expended during this problem identification and resolution inspection were reduced by approximately 50 percent.

The NRC inspection team reviewed the stations corrective action program and the stations implementation of the program to evaluate its effectiveness in identifying, prioritizing, evaluating, and correcting problems, and to confirm that the station was complying with NRC regulations and licensee standards for corrective action programs. Based on the samples reviewed, the team determined that your staffs performance in each of these areas adequately supported nuclear safety.

The team also evaluated the stations processes for use of industry and NRC operating experience information and the effectiveness of the stations audits and self-assessments.

Based on the samples reviewed, the team determined that your staffs performance in each of these areas adequately supported nuclear safety.

Finally, the team reviewed the stations programs to establish and maintain a safety-conscious work environment (SCWE) and interviewed station personnel to evaluate the effectiveness of these programs. This review was also a follow-up to the NRC Confirmatory Order (CO) EA-17-022, dated July 27, 2017 (ML17208A647). Based on the teams reviews, observations, and the results of these interviews, the team found no evidence of challenges to your organizations safety-conscious work environment. Your employees appeared willing to raise nuclear safety concerns through at least one of the several means available. No NRC-identified or self-revealing findings were identified during this inspection. However, NRC inspectors identified one Severity Level IV violation with no associated finding. The NRC is treating this violation as a non-cited violation (NCV) consistent with Section 2.3.2.a of the Enforcement Policy.

If you contest the violation or significance or severity of the violation documented in this inspection report, you should provide a response within 30 days of the date of this inspection report, with the basis for your denial, to the U.S. Nuclear Regulatory Commission, ATTN:

Document Control Desk, Washington, DC 20555-0001; with copies to the Regional Administrator, Region II; the Director, Office of Enforcement; and the NRC Resident Inspector at Sequoyah.

This letter, its enclosure, and your response (if any) will be made available for public inspection and copying at http://www.nrc.gov/reading-rm/adams.html and at the NRC Public Document Room in accordance with 10 CFR 2.390, Public Inspections, Exemptions, Requests for Withholding.

Sincerely,

/RA/

Omar R. López-Santiago, Chief Reactor Projects Branch 5 Division of Reactor Projects

Docket Nos.: 05000327 and 05000328 License Nos.: DPR-77 and DPR-79

Enclosure:

As stated

Inspection Report

Docket Numbers:

05000327 and 05000328

License Numbers:

DPR-77 and DPR-79

Report Numbers:

05000327/2019011 and 05000328/2019011

Enterprise Identifier: I-2019-011-0036

Licensee:

Tennessee Valley Authority

Facility:

Sequoyah Nuclear Plant, Units 1 and 2

Location:

Soddy-Daisy, TN 37379

Inspection Dates:

June 03, 2019 to June 27, 2019

Inspectors:

J. Seat, Project Engineer

M. Checkle, Senior Allegations Coordinator

N. Childs, Resident Inspector

W. Deschaine, Project Engineer

Approved By:

Omar R. López-Santiago, Chief

Reactor Projects Branch 5

Division of Reactor Projects

SUMMARY

The U.S. Nuclear Regulatory Commission (NRC) continued monitoring the licensees performance by conducting a biennial problem identification and resolution inspection at Sequoyah Nuclear Plant, Units 1 and 2, in accordance with the Reactor Oversight Process. The Reactor Oversight Process is the NRCs program for overseeing the safe operation of commercial nuclear power reactors. Refer to https://www.nrc.gov/reactors/operating/oversight.html for more information.

List of Findings and Violations

Failure to Adequately Implement Requirements of Confirmatory Order EA-17-022,

Commitment V.1.b.3 Cornerstone Significance Cross-Cutting Aspect Report Section Not Applicable NCV 05000327,05000328/2019011-

Open/Closed Not Applicable 92702 The inspectors identified a Severity Level IV NCV for the licensees failure to adequately implement requirements of Confirmatory Order (CO) EA-17-022, Commitment V.1.b.3. Specifically, the licensee failed to ensure that new supervisory employees completed safety conscious work environment (SCWE) training within three months of their hire or promotion effective date.

Additional Tracking Items

None

INSPECTION SCOPES

Inspections were conducted using the appropriate portions of the inspection procedures (IPs) in effect at the beginning of the inspection unless otherwise noted. Currently approved IPs with their attached revision histories are located on the public website at http://www.nrc.gov/reading-rm/doc-collections/insp-manual/inspection-procedure/index.html. Samples were declared complete when the IP requirements most appropriate to the inspection activity were met consistent with Inspection Manual Chapter (IMC) 2515, Light-Water Reactor Inspection Program - Operations Phase. The inspectors reviewed selected procedures and records, observed activities, and interviewed personnel to assess licensee performance and compliance with Commission rules and regulations, license conditions, site procedures, and standards.

OTHER ACTIVITIES - BASELINE

71152B - Problem Identification and Resolution Biennial Team Inspection (IP Section 02.04)

The inspectors performed a biennial assessment of the licensees corrective action program, use of operating experience, self-assessments and audits, and safety conscious work environment.

  • Corrective Action Program Effectiveness: The inspectors assessed the corrective action programs effectiveness in identifying, prioritizing, evaluating, and correcting problems.
  • Operating Experience, Self-Assessments and Audits: The inspectors assessed the effectiveness of the stations processes for use of operating experience, audits and self-assessments.
  • Safety Conscious Work Environment: The inspectors assessed the effectiveness of the stations programs to establish and maintain a safety-conscious work environment.

OTHER ACTIVITIES

- TEMPORARY INSTRUCTIONS, INFREQUENT AND ABNORMAL

92702 CONF - Enforcement Related Order Follow-Up-Only Enforcement Related Order Follow-Up-Only

The inspectors reviewed commitments associated with four items from Confirmatory Order EA-17-022, issued to TVA on July 27, 2017.

(1) Commitment V.1.b.2: This commitment and action required that training be provided within one year and on an annual basis thereafter to, at a minimum, all working status nuclear business group supervisory employees, contractor supervisory employees involved in nuclear-related work activities, human resource staff involved in the adverse employment action process, employee concerns program staff, contract technical stewards for nuclear-related work activities, and the personnel in the TVA Office of General Counsel who are engaged in nuclear-related work activities. TVA identified 419 individuals at Sequoyah and TVA Corporate who were required to complete the training. The inspectors verified that the list of individuals included first line supervisors and above, contract technical stewards, human resources personnel, and employee concerns program personnel. The inspection was only completed for Sequoyah and TVA Corporate.
(2) Commitment V.1.b.3: This commitment and action required that new supervisory employees complete initial training through in-person or computer-based training within three months of their hire or promotion effective date. The training also required, at a minimum, a discussion of the training material with personnel in the TVA Office of General Counsel who are engaged in nuclear-related work activities. This commitment applied to new supervisory employees who were not included in the initial training specified in Commitment V.1.b.2. The inspectors reviewed records of Sequoyah and TVA Corporate employees and contractors who were hired or promoted into supervisory positions after July 28, 2018, to verify that personnel had completed the specified training within three months of their hire or promotion effective date. The inspection was only completed for Sequoyah and TVA Corporate.
(3) Commitment V.1.d.1: Inspectors performed an independent review of recent Adverse Employment Action and Executive Review Board (ERB) packages at Sequoyah and TVA Corporate. Specific activities included review of the background information associated with recent ERBs, associated SCWE Mitigation Plan Screening, SCWE Mitigation Plans, and results of recent pulse surveys conducted as a result of adverse actions taken against employees. The inspection was only completed for Sequoyah and TVA Corporate.
(4) Commitment V.1.e.1: This commitment required TVA to conduct an independent nuclear safety culture (NSC) assessment at Sequoyah and TVA Corporate by July 2018, evaluate the results and develop, implement, and track to completion, corrective actions to address weaknesses identified through the assessment. The inspectors reviewed corrective actions and enhancements associated with the 2018 nuclear safety culture assessments at Sequoyah (CR 1404011) and TVA Corporate (CR 1416534) to verify that corrective actions were implemented and tracked to completion. The inspection was only completed for Sequoyah and TVA Corporate.

INSPECTION RESULTS

Assessment 71152B

1. Corrective Action Program Effectiveness

Based on the samples reviewed, the team determined that the licensees corrective action program (CAP) complied with regulatory requirements and self-imposed standards. The licensees implementation of the CAP adequately supported nuclear safety.

Problem Identification: The team determined that most conditions that required generation of a condition report (CR) by licensee procedure, NPG-SPP-22.300, Corrective Action Program, had been appropriately entered into the CAP. The team observed members at the Management Review Committee (MRC) and Plant Screening Committee (PSC) meetings appropriately questioning and challenging condition reports to ensure clarification of issues and appropriate entry into the CAP. Based on the samples reviewed, the team determined that the licensee trended equipment and programmatic issues, and appropriately identified problems in condition reports. Additionally, the team concluded that personnel were identifying trends at low levels. The inspectors performed walkdowns, reviewed CRs, and reviewed system health and trending reports for the Auxiliary Feedwater System (AFW) and Chemical and Volume Control System (CVCS). Based on the inspectors' reviews and walkdowns of accessible portions of those systems, the inspectors determined that deficiencies were being identified and placed in the CAP. Overall, the team determined that the licensee is identifying problems at the proper threshold and entering them into the corrective action program.

Problem Prioritization and Evaluation: Based on the review of corrective action documents sampled by the inspection team during the onsite period, the team concluded that problems were generally prioritized and evaluated in accordance with the licensees CAP procedures as described in NPG-SPP-22.300, Corrective Action Program." Operability and reportability determinations were performed when conditions warranted, and the evaluations generally supported the conclusions. The causal analyses reviewed, appropriately considered the extent of condition or problem, generic issues, and previous occurrences of the issue. In general, the team determined the technical adequacy and depth of evaluations was appropriate. The team noted that the documented justification for extending some corrective action due dates lacked detail, however, the extensions appeared acceptable based on the nature of the corrective action. Overall, the team determined that the licensees process for evaluating and prioritizing issues once they had been entered into the corrective action program supported nuclear safety.

Effectiveness of Corrective Actions: Based on a review of corrective action documents, interviews with licensee staff, and verification of completed corrective actions, the inspectors determined that corrective actions were timely, commensurate with the safety significance of the issues, and effective, in that conditions adverse to quality were corrected. For significant conditions adverse to quality, the corrective actions directly addressed the cause and effectively prevented recurrence. The inspectors reviewed condition reports and effectiveness reviews to verify that the significant conditions adverse to quality had not recurred. Effectiveness reviews for corrective actions to preclude repetition were generally sufficient to ensure corrective actions were properly implemented and were effective. The inspectors reviewed corrective action documents for NRC findings issued since the last problem identification & resolution (PI&R) biennial inspection. The team determined that corrective actions completed or planned were adequate to address the NRC findings, and completion dates for open actions were reasonable.

2. Use of Operating Experience (OE)

Based on a review of selected documentation related to operating experience issues, the team determined that the licensee was generally effective in screening industry and NRC OE for applicability to the plant. Industry OE was evaluated at either the corporate or plant level depending on the source and type of document. Relevant information was forwarded to the applicable department for further action or informational purposes. Operating experience issues requiring action were entered into the CAP for tracking and closure. The team determined that the licensee's use of industry and NRC OE was effective, and the program adequately supported nuclear safety. The team did note that procedural requirements related to OE screening timeliness were vague, however, the team did not identify any instances where OE was not screened in a timely manner.

3. Self-Assessments and Audits

The team determined that the scopes of assessments and audits were adequate. Self-assessments were generally detailed and critical. The team verified that CRs were created to document areas for improvement and findings resulting from self-assessments, and verified that actions had been completed consistent with those recommendations. Audits of the quality assurance program appropriately assessed performance and identified areas for improvement. Generally, the licensee performed evaluations that were technically accurate.

4. Safety Conscious Work Environment

Based on a sample size of approximately 35 individuals, interviewed from a cross-section of plant employees at Sequoyah and the TVA Corporate office, the team found no evidence of challenges to a safety-conscious work environment at either location. The following departments were sampled: Nuclear Oversight - Quality Assurance (52% sample),

Maintenance (12% sample), Chemistry (6% sample), Radiation Protection (8% sample),

Emergency Preparedness (6% sample), and Licensing (15% sample). Employees interviewed were willing to raise nuclear safety concerns through at least one of the several means available.

Interviewees were asked a series of questions in a semi-structured interview format.

Follow-up questions were asked as necessary to facilitate a full understanding of employees perceptions of the work environment. Questions included:

  • Do you feel like your department encourages people to raise nuclear, radiological, or regulatory safety concerns (including challenging actions or decisions believed to be unsafe)?
  • Do you feel like you can raise nuclear, radiological, or regulatory safety concerns safety concerns without fear of retaliation?
  • Are you aware of any instance where someone experienced a negative reaction from a supervisor or manager for raising a nuclear, radiological, or regulatory safety issue?
  • Do you believe other employees may be hesitant to raise nuclear, radiological, or regulatory safety concerns? Why? What would make them hesitant?
  • Do you believe management is aware of these issues? Have actions been taken to address the situation?
  • If you did not feel comfortable using your chain of command, are there other avenues you would use to raise a nuclear safety concern?
  • In the past 6 months, has the environment in your department gotten better, worse, stayed the same?
  • Would you feel comfortable using the Employee Concerns Program (ECP) if you had a nuclear safety concern?
  • Do you feel like you are able to be open when participating in ECP pulsing surveys or other work environment assessments?
  • Are you aware of the proposed changes regarding the ECP program at TVA?
  • Do you feel like the new ECP structure would still provide independence from management?

Prior to the inspection, the licensee made fleet-wide communications regarding proposed changes to the ECP. When queried about the proposed ECP changes during the interviews, 31% of those interviewees were concerned that the proposed structure of the ECP would not provide independence from management, however, most would still be willing to use the ECP.

Minor Violation 71152B Minor Violation: 10 CFR 50, Appendix B, Criterion V, "Instructions, Procedures, and Drawings," states, in part, "Activities affecting quality shall be prescribed by documented instructions, procedures, or drawings, of a type appropriate to the circumstances and shall be accomplished in accordance with these instructions, procedures, or drawings."

Contrary to the above, on August 15, 2017, the licensee failed to accomplish activities affecting quality in accordance with established procedures. Specifically, the licensee did not follow procedure NPG-SPP-22.300, "Corrective Action Program," Revision 9, step 3.7.6.B.1, which requires that corrective action controls (CA Control Flag in Maximo) be applied to work orders (WOs) credited for closure of a condition report requiring corrective actions. CR 1313355, which documented undersized seismic restraints securing temporary equipment, was closed to WO 118888040 without applying the required corrective action controls. WO 118888040 was later closed without sufficient evidence to demonstrate that appropriate actions had been taken to correct the condition identified in CR 1313355. The failure to apply corrective action controls to WO 118888040, per NPG-SPP-22.300, was a performance deficiency.

Screening: The inspectors determined the performance deficiency was minor. The inspectors answered "no" to the more than minor screening questions in IMC 0612 Appendix B, "Issue Screening," dated January 1, 2018.

Enforcement:

The licensee initiated CR 1526428 to address this minor violation. The licensee performed walkdowns to verify that temporary equipment secured with undersized seismic restraints was no longer present. This failure to comply with procedural requirements constitutes a minor violation that is not subject to enforcement action in accordance with the NRCs Enforcement Policy.

Failure to Adequately Implement Requirements of Confirmatory Order EA-17-022, Commitment V.1.b.3 Cornerstone Severity Cross-Cutting Aspect Report Section Not Applicable Severity Level IV NCV 05000327,05000328/2019011-01 Open/Closed

Not Applicable 92702 The inspectors identified a Severity Level (SL) IV NCV for the licensees failure to adequately implement requirements of Confirmatory Order EA-17-022, Commitment V.1.b.3. Specifically, the licensee failed to ensure that new supervisory employees completed safety conscious work environment (SCWE) training within three months of their hire or promotion effective date.

Description:

Confirmatory Order (CO) EA-17-022, issued to TVA on July 27, 2017, requires, in part, that certain personnel complete initial and recurring SCWE training. Specifically, commitment V.1.b.3 in CO EA-17-022 requires that: New supervisory employees shall complete initial training through in-person or computer-based training within three months of their hire or promotion effective date. The training shall require, at a minimum, a discussion of the training material with personnel in the TVA Office of General Counsel who are engaged in nuclear related work activities.

On December 26, 2018, the licensee identified two nuclear business group employees and one contractor employee at Sequoyah who were hired into or promoted to supervisory positions after July 27, 2018, but who did not complete the specified SCWE training within three months of their hire or promotion effective date. The licensee entered this issue into their CAP as CR 1478023. At the time this CR was written, the licensee did not realize that this training requirement was also applicable to supplemental workers.

In March of 2019, at an NRC Inspection Exit Meeting at Watts Bar, TVA was notified that the 90-day SCWE requirement does apply to supplemental workers. The licensee completed an extent of condition review and identified four contractor employees involved in nuclear related work activities who were new to supervisory positions and did not complete the training in the three-month time period.

Corrective Actions: The licensee entered this issue into their corrective action program on December 26, 2018 and took immediate action to ensure all Sequoyah employees had completed the training by February 6, 2019. A CR was written on December 26, 2018, with actions to perform an apparent cause analysis of the incorrect due dates and track actions at the TVA Corporate level. The licensee initiated a CR on March 5, 2019, to document the missed SCWE training for new contractor supervisory employees.

Corrective Action References: CR 1477482, CR 1477964, CR 1484364, CR 1478023, CR 1497144

Performance Assessment:

The licensees failure to ensure that new supervisory employees completed SCWE training within three months of their hire or promotion effective date was in violation of commitment V.1.b.3 in Confirmatory Order Modifying License (EA-17-022). The inspectors determined that this violation was associated with impeding the regulatory process and subject to traditional enforcement as described in the NRC Enforcement Policy, dated May 15, 2019.

Enforcement:

The ROPs significance determination process does not specifically consider the regulatory process impact in its assessment of licensee performance. Therefore, it is necessary to address this violation which impedes the NRCs ability to regulate using traditional enforcement to adequately deter non-compliance.

Severity: The inspectors determined this violation constituted a more than minor traditional enforcement violation associated with failure to implement the requirements of CO EA-17-022. The inspectors determined that the failure to ensure that current and future CO requirements continue to be met could potentially impact safety. Specifically, in this example, failure to ensure new supervisory employees complete SCWE training in a timely manner could cause missed opportunities to identify and/or prevent an environment where individuals would be hesitant to raise nuclear safety concerns for fear of retaliation. The violation is more than minor because it was not isolated to one or two individuals. The inspectors determined that the licensees failure to implement the requirements of the Confirmatory Order is considered an SL IV violation, consistent with Section 2.2.2.d of the NRC Enforcement Policy, dated May 28, 2019.

Violation: Commitment V.1.b.3 in Confirmatory Order EA-17-022, issued to TVA on July 27, 2017, requires, in part, that: New supervisory employees shall complete initial training through in-person or computer-based training within three months of their hire or promotion effective date. The training shall require, at a minimum, a discussion of the training material with personnel in the TVA Office of General Counsel who are engaged in nuclear related work activities.

Contrary to the above, from July 28, 2018 to March 5, 2019, the licensee failed to ensure that new supervisory employees completed SCWE training within three months of their hire or promotion effective date. Specifically, two new Sequoyah supervisory employees and five new contractor supervisory employees involved in nuclear related work activities did not complete the SCWE training within three months as required.

Enforcement Action: This violation is being treated as a non-cited violation, consistent with Section 2.3.2 of the Enforcement Policy.

EXIT MEETINGS AND DEBRIEFS

The inspectors verified no proprietary information was retained or documented in this report.

  • On June 20, 2019, the inspectors presented the biennial problem identification and resolution inspection results to Mr. Matthew Rasmussen and other members of the licensee staff.
  • On June 27, 2019, the inspectors presented the confirmatory order follow-up inspection results to Mr. Matthew Rasmussen and other members of the licensee staff.

DOCUMENTS REVIEWED

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

71152B

Calculations

MDQ0000682018000101 Material Aging for PORV Target Rock Solenoid Valves

(SQNEQ-SOL-002)

Revision 0

71152B

Calculations

SCG1S596

Maintenance Rule for Structures and License Renewal

Structures Monitoring Program Inspections

Revision 13

71152B

Corrective Action

Documents

CR 1002259

OE - Foreign Material Damages Steam Generator

Tube Sheet

03/20/2015

71152B

Corrective Action

Documents

CR 1002268

OE - Performance Shortfalls During Mechanical

Maintenance Activities

03/20/2015

71152B

Corrective Action

Documents

CR 1002270

NOER - Loss of Breaker Configuration Control PER

965728

03/20/2015

71152B

Corrective Action

Documents

CR 1002275

NOER - Missed Surveillance on New Components

03/20/2015

71152B

Corrective Action

Documents

CR 1002293

OE - Loss of Jet Pump Plug Seals in Reactor Vessel

03/20/2015

71152B

Corrective Action

Documents

CR 1003153

OE - BFN Loss of Inventory from Reactor Cavity

03/23/2015

71152B

Corrective Action

Documents

CR 1017143

Found Cracks in the Cover on Vital Battery #2

04/22/2015

71152B

Corrective Action

Documents

CR 1023172

NOER - Reactor Trip due to Loss of Main Condenser

Vacuum

05/07/2015

71152B

Corrective Action

Documents

CR 1023175

NOER - PER Classification and Level of Significance

05/07/2015

71152B

Corrective Action

Documents

CR 1023207

OE - Ice Bed Increasing Temperature Trends

05/07/2015

71152B

Corrective Action

Documents

CR 1025764

Oil Bubbler is at 20% Recommend Minor Maintenance

to Fill Reservoir

05/14/2015

71152B

Corrective Action

Documents

CR 1064736

Evaluate DCN 23085 - Kirk Key Interlocks

07/30/2015

71152B

Corrective Action

Documents

CR 1084294

NRC NCV 2015-007-02 - 50.59/Modifications

Inspection

09/21/2015

71152B

Corrective Action

Documents

CR 1104335

CRDM Cable Connection Issues Found During

Disconnection

11/15/2015

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

71152B

Corrective Action

Documents

CR 1106765

1-LCV-3-148 not Able to be Operated in Manual

11/20/2015

71152B

Corrective Action

Documents

CR 1116558

2-FSV-43-55 Failed 2-SI-SXV-000-204.0 Valve Stroke

2/16/2015

71152B

Corrective Action

Documents

CR 1121723

2-FSV-43-61 Has no Light Indication While Valve is

Closed

01/05/2016

71152B

Corrective Action

Documents

CR 115765

Potential Transformer (PT) in Compartment #3

2/01/2006

71152B

Corrective Action

Documents

CR 1169090

Post Accident Monitoring (2-XX-55-6L) for Valve 2-

FCV-43-61 Indicates Intermediate Position

05/09/2016

71152B

Corrective Action

Documents

CR 1181710

NRC CDBI DG Bldg Ventilation System and Tornado

Impact

06/14/2016

71152B

Corrective Action

Documents

CR 1187308

Operations Request POE - Instrument Calibration

Issues

06/30/2016

71152B

Corrective Action

Documents

CR 1227157

Potential Error Trap with Breaker UNIDs

10/26/2016

71152B

Corrective Action

Documents

CR 1240813

0-MI-MRR-003-461.0 Needs to be Revised - TDAFW

Mech Overspeed Trip Linkage Spring Setting is

Incorrect

2/10/2016

71152B

Corrective Action

Documents

CR 1254470

CRs Closed to WOs Without Correct Coding in WO

01/25/2017

71152B

Corrective Action

Documents

CR 1254937

NOER was not Generated for CR 1241933

01/26/2017

71152B

Corrective Action

Documents

CR 1255171

Gaps in Extent of Condition Review of QA Finding

RCA 1155352

01/26/2017

71152B

Corrective Action

Documents

CR 1255177

Trend in Site CAP Procedure Adherence to NPG-SPP-

2.300

01/26/2017

71152B

Corrective Action

Documents

CR 1269767

A212 ABSCE Breach Resulting in Both Trains of

ABGTS Inoperable for Both Units

03/07/2017

71152B

Corrective Action

Documents

CR 1290969

Snapshot Assessment - PD - SQN-PI-SSA-17-007 -

OE Coordinators

05/02/2017

71152B

Corrective Action

Documents

CR 1301718

Unit 1 TDAFW Suction Pressure Gauge Found

Isolated

05/30/2017

71152B

Corrective Action

CR 1303852

RP REP VANS

06/05/2017

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

Documents

71152B

Corrective Action

Documents

CR 1305710

Procedure Change Request for 2-SI-SXV-003-219.S

06/10/2017

71152B

Corrective Action

Documents

CR 1311223

QA ID: The Chemical Hygiene Plan was not reviewed

during 2016 (SSA1707)

06/26/2017

71152B

Corrective Action

Documents

CR 1311501

QA ID: SSA1707: Inconsistent performance of

surveillance procedure requirements

06/27/2017

71152B

Corrective Action

Documents

CR 1313355

Inadequate chain size used for temporary equipment

seismic restraint

07/03/2017

71152B

Corrective Action

Documents

CR 1313866

OE-Green-WBN-NOER-17-014-Unplanned LCO 3.7.5

entry due to time delay relay failure

07/05/2017

71152B

Corrective Action

Documents

CR 1321168

Corrective Action for CR 1303852 did not resolve

condition identified

07/25/2017

71152B

Corrective Action

Documents

CR 1323549

QAID Improper use of N/A (SSA 1708)

08/01/2017

71152B

Corrective Action

Documents

CR 1323551

QA Records from ALARA not being transmitted to

EDMS

08/01/2017

71152B

Corrective Action

Documents

CR 1323555

QAID Temporary Shielding forms not properly filled out

(SSA 1708)

08/01/2017

71152B

Corrective Action

Documents

CR 1323558

QAID Recommendation on temporary shielding

support (SSA 1708)

08/01/2017

71152B

Corrective Action

Documents

CR 1324371

Follow-up on CR 1324282 from SQN RP - RW Audit

08/03/2017

71152B

Corrective Action

Documents

CR 1334122

NRC Regulatory Issue Summary (RIS) 2017-04

08/31/2017

71152B

Corrective Action

Documents

CR 1336290

Cable Tray Supports out of Tolerance

09/07/2017

71152B

Corrective Action

Documents

CR 1341686

Cable Tray Supports out of Tolerance

09/25/2017

71152B

Corrective Action

Documents

CR 1343410

SGI records

09/29/2017

71152B

Corrective Action

Documents

CR 1364616

OE - Part 21 2017-52-00 Fisher Type 461 Valve Plug

Machining

2/04/2017

71152B

Corrective Action

CR 1366082

SQN DBA EQ 201700X

2/07/2017

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

Documents

71152B

Corrective Action

Documents

CR 1366200

Unit 1 Lower Compartment Cooler Motor EQ

Qualification

2/072017

71152B

Corrective Action

Documents

CR 1372336

Fatigue Rule Violation

2/28/2017

71152B

Corrective Action

Documents

CR 1378392

M-B ERCW Pump stopped due to rising bearing temps

01/18/2018

71152B

Corrective Action

Documents

CR 1380592

Equipment relocated during installation of plexi-glass

01/24/2018

71152B

Corrective Action

Documents

CR 1381347

NCV 2017008-01, Unjustified Qualified Life for Target

Rock PORVs

01/26/2018

71152B

Corrective Action

Documents

CR 1381348

NCV 2017008-02, Inadequate Qualification for Reactor

Lower Compartment Cooler Motors

01/26/2018

71152B

Corrective Action

Documents

CR 1391505

Deficiencies identified during mock 95001 inspection

2/28/2018

71152B

Corrective Action

Documents

CR 1394115

OE - NRC Information Notice 2018-02

03/08/2018

71152B

Corrective Action

Documents

CR 1403173

Boric acid valve leaking badly near BAT pump 1A

04/09/2018

71152B

Corrective Action

Documents

CR 1403747

SGI Records

04/09/2018

71152B

Corrective Action

Documents

CR 1403761

SGI Records

04/09/2018

71152B

Corrective Action

Documents

CR 1403896

Boric acid leak on Unit 2 emergency boration FT

instrument line

04/10/2018

71152B

Corrective Action

Documents

CR 1403944

SGI Records

04/10/2018

71152B

Corrective Action

Documents

CR 1403950

SGI Records

04/11/2018

71152B

Corrective Action

Documents

CR 1404549

1-LT-62-130 VCT Level Indication Failed Low

04/11/2018

71152B

Corrective Action

Documents

CR 1404590

LL BOP/NSSS DCS Loss of 62-130A

04/11/2018

71152B

Corrective Action

CR 1407364

U1R22 Outage WO Screening - FIN resources

04/20/2018

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

Documents

71152B

Corrective Action

Documents

CR 1408522

Issues found during performance of 1-SI-SXP-062-

203.0

04/24/2018

71152B

Corrective Action

Documents

CR 1408611

Troubleshoot CCP 1A Pump Vibration After U1R22

Rebuild

04/24/2018

71152B

Corrective Action

Documents

CR 1410388

Grout base plate under 1A CCP post U1R22

05/01/2018

71152B

Corrective Action

Documents

CR 1413732

Non-cited Violation (NCV) 05000327/328/2018001-01

05/11/2018

71152B

Corrective Action

Documents

CR 1413734

Non-cited Violation (NCV) 05000327/328/2018001-02

05/11/2018

71152B

Corrective Action

Documents

CR 1414850

NRC Identified Green NCV 390/2018410

05/15/2018

71152B

Corrective Action

Documents

CR 1416612

Vibration Point 8H in Alert Range

05/21/2018

71152B

Corrective Action

Documents

CR 1433166

Suspect B Train EGTS FS-65-44 Failed

07/22/2018

71152B

Corrective Action

Documents

CR 1436225

EGTS Licensee Event Report Required Information

08/02/2018

71152B

Corrective Action

Documents

CR 1443992

OE - Review NRC IN 18-09 Electrical Arc Flash

08/30/2018

71152B

Corrective Action

Documents

CR 1444099

Found leads lifted for an alarm on 1B diesel

08/31/2018

71152B

Corrective Action

Documents

CR 1447183

OE - IN-18-10, Thermal Sleeve Flange Wear Leads to

Stuck Control Rod

09/13/2018

71152B

Corrective Action

Documents

CR 1449176

OE - NRC Regulatory Issue Summary 2018-04

09/20/2018

71152B

Corrective Action

Documents

CR 1463962

Inability to timely retrieve design records

11/07/2018

71152B

Corrective Action

Documents

CR 1471007

EQ Binder SQN-SOL-002 baseline evaluation

11/29/2018

71152B

Corrective Action

Documents

CR 1476565

Minor Void Found in Emergency Boration Line Above

1-FT-62-137

2/18/2018

71152B

Corrective Action

CR 1477034

Gas void observed during performance of 1-SI-OPS-

2/19/2018

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

Documents

2-040.A U1 CCP piping vent

71152B

Corrective Action

Documents

CR 1482178

SQN Site Records List does not agree with NPG-SPP-

2.300 records (QA audit SSA1901)

01/14/2019

71152B

Corrective Action

Documents

CR 1482468

QA ID: Department OE Coordinators have not

completed the required JFG (SSA1901)

01/15/2019

71152B

Corrective Action

Documents

CR 1482669

Biennial fleet wide self assessment of the OE program

not performed as required by NPG-SPP-22.500

01/15/2019

71152B

Corrective Action

Documents

CR 1483225

Revision recommendation for NPG-SPP-22.300

01/17/2019

71152B

Corrective Action

Documents

CR 1483228

Revision recommendation for NPG-SPP-22.500

01/17/2019

71152B

Corrective Action

Documents

CR 1483291

Re-evaluate NPG-SPP-22.500 as quality related

01/17/2019

71152B

Corrective Action

Documents

CR 1485069

2019 WBN PI&R Inspection - Issues with CR 1414850

01/24/2019

71152B

Corrective Action

Documents

CR 1488033

Non-cited Violation (NCV) 2018004-02

2/04/2019

71152B

Corrective Action

Documents

CR 1489420

Revise security procedure

2/08/2019

71152B

Corrective Action

Documents

CR 1490857

Rx Power Does not Respond Correctly to Manual

Make-ups Calculated to Maintain Power Stable

2/14/2019

71152B

Corrective Action

Documents

CR 1490951

Evaluation of trend intrusion issues in manholes across

SQN

2/14/2019

71152B

Corrective Action

Documents

CR 1491065

Establish and sustain a culture of excellence in PU&A

in Chemistry

2/14/2019

71152B

Corrective Action

Documents

CR 1494149

OE - WBN Integrated Inspection Report Nov 2018

Findings

2/27/2019

71152B

Corrective Action

Documents

CR 1498586

DCN 21287 contained an incorrect calculation for main

steam line radiation release rate

03/13/2019

71152B

Corrective Action

Documents

CR 1500107

SQN-PI-FSA-19-002, PI&R Self Assessment

03/18/2019

71152B

Corrective Action

Documents

CR 1500629

OE - IN-2019-01, Inadequate Evaluation of Temporary

Alterations

03/20/2019

71152B

Corrective Action

CR 1503036

2017 SQN EQ DBA Inspection: Foxboro/Weed

03/28/2019

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

Documents

Transmitter heat rise issue, SLD.

71152B

Corrective Action

Documents

CR 1503045

2017 SQN EQ DBA Inspection: ASCO valves potential

performance deficiencies, SLD

03/28/2019

71152B

Corrective Action

Documents

CR 1503045

2017 SQN EQ DBA Inspection - ASCO valves potential

performance deficiencies

03/28/2019

71152B

Corrective Action

Documents

CR 1506308

Non-cited Violation (NCV) 2018412-01

04/09/2019

71152B

Corrective Action

Documents

CR 1506325

Replace U1 LCC Fan Motors during U1R24

04/09/2019

71152B

Corrective Action

Documents

CR 1506831

Review Unusual Event at Brunswick Unit 1 which

required a shutdown

04/10/2019

71152B

Corrective Action

Documents

CR 1509174

Respond to NRC RIS 2019-02, Preparation and

Scheduling of Operator Licensing Examinations

04/18/2019

71152B

Corrective Action

Documents

CR 1510339

SQN-PI-FSA-10-002 - Objective 7 - Appendix R

Triennial Inspection CR 1276596 has not been

resolved timely

04/23/2019

71152B

Corrective Action

Documents

CR 1510464

CR 1485069 did not document department manager

approval

04/23/2019

71152B

Corrective Action

Documents

CR 1510873

SQN-PI-FSA-19-002 - Objective 7 - Deficiencies noted

in CRs 1403944, 1441458, and 1403761

04/24/2019

71152B

Corrective Action

Documents

CR 1510985

SQN-PI-FSA-!(-002 - Objective 7 PD - A Review of

NCV 2017008-01

04/24/2019

71152B

Corrective Action

Documents

CR 1511003

SQN-PI-FSA-19-002 - Objective 7 PD - A Review of

NCV 2017008-02

04/24/2019

71152B

Corrective Action

Documents

CR 1511249

SQN-PI-FSA-19-002 Objective 7 PD (1500107-033)

LER-2018-001-00

04/25/2019

71152B

Corrective Action

Documents

CR 1512747

Non-cited Violation (NCV) 05000327/328/2019010-01

05/01/2019

71152B

Corrective Action

Documents

CR 1514352

QA elevation on protected equipment

05/06/2019

71152B

Corrective Action

Documents

CR 1516824

NCV 2019-02, Failure to account for heat rise in

Foxboro/Weed instruments

05/15/2019

71152B

Corrective Action

Documents

CR 1519228

Gas/water Flow Noted During Cold Leg Injection Piping

Vent

05/23/2019

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

71152B

Corrective Action

Documents

CR 1525798

OE - Issues with OE Reviews in Accordance with

NPG-SPP-22.600

06/18/2019

71152B

Corrective Action

Documents

CR 655554

Loop 4 TDAFW LCV failed stroke time

2/12/2012

71152B

Corrective Action

Documents

CR 660015

OE review of WBN-NOER-12-079

2/21/2012

71152B

Corrective Action

Documents

CR 663698

Review of WBN-NOER-12-106 AFW valve stroke time

01/04/2013

71152B

Corrective Action

Documents

CR 740635

SGTR accident analysis issue related to maintenance

06/14/2013

71152B

Corrective Action

Documents

CR 750649

SQN review of Byron U2 scram from loss of main

generator stator cooling

07/09/2013

71152B

Corrective Action

Documents

CR 751276

SQN review of Vogtle U2 manual reactor scram due to

high RCP seal leak off

07/10/2013

71152B

Corrective Action

Documents

CR 791573

SQN review of Davis-Besse scram from RCP motor

faulty electrical connections

10/10/2013

71152B

Corrective Action

Documents

CR 915358

Unit 2 main turbine high vibration

07/30/2014

71152B

Corrective Action

Documents

CR 959976

Aging management review for ground water in

distribution board

11/24/2014

71152B

Corrective Action

Documents

CR 965728

Procedure swap performed with step marked N/A that

resulted in configuration control issue

2/10/2014

71152B

Corrective Action

Documents

CR 973446

2B MDAFW system check valve backleakage

01/05/2015

71152B

Corrective Action

Documents

CR 981733

Low oil on 2A MDAFWP inboard pump bearing

01/27/2015

71152B

Corrective Action

Documents

Resulting from

Inspection

CR 1522084

Broken UNID tag

06/04/2019

71152B

Corrective Action

Documents

Resulting from

Inspection

CR 1522525

Procedure NPG-SPP-22.300 change request

06/05/2019

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

71152B

Corrective Action

Documents

Resulting from

Inspection

CR 1525710

Individual missed 2018 SCWE Training - CO issue

06/18/2019

71152B

Corrective Action

Documents

Resulting from

Inspection

CR 1525830

NRC ID - ERB package documentation error - CO

issue

06/18/2019

71152B

Corrective Action

Documents

Resulting from

Inspection

CR 1525832

NPG-SPP-03.9 wording of Significant Gap Analysis not

matching NPG-SPP-22.300

06/18/2019

71152B

Corrective Action

Documents

Resulting from

Inspection

CR 1525869

NOER-SQN-17-003 has incorrect event date

06/18/2019

71152B

Corrective Action

Documents

Resulting from

Inspection

CR 1526184

Extension request reason insufficient

06/19/2019

71152B

Corrective Action

Documents

Resulting from

Inspection

CR 1526337

Incorrect Maximo attachments

06/20/2019

71152B

Corrective Action

Documents

Resulting from

Inspection

CR 1526428

Inadequate response to CRs

06/20/2019

71152B

Engineering

Changes

DCN 23813

Replace Steam Generator Blowdown Containment

Isolation Sample Valves

Revision 1

71152B

Miscellaneous

U2 Function 043-E (a)(1) plan

Revision 2

71152B

Miscellaneous

Quality Assurance Master Audit Schedule 2019-2020

08/29/2017

71152B

Miscellaneous

Browns Ferry Nuclear Plant, Sequoyah Nuclear Plant,

and Watts Bar Nuclear Plant Initial Response to NRC

05/09/2008

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

Generic Letter 2008-01

71152B

Miscellaneous

Sequoyah Nuclear Plant - Closeout of Generic Letter 2008-01

04/22/2011

71152B

Miscellaneous

Operations Standing Order List

06/05/2019

71152B

Miscellaneous

Chemical and Volume Control System (CVCS) Health

Report Scorecard

1st Quarter

2019

71152B

Miscellaneous

SQN Maintenance Rule List - SSCs in (a)(1) Status

since June 2017

71152B

Miscellaneous

Unit 1 MCR Deficiencies List

06/05/2019

71152B

Miscellaneous

Unit 2 MCR Deficiencies List

06/05/2019

71152B

Miscellaneous

System #333 Health Report Screenshot

71152B

Miscellaneous

CDE 2855

2-FSV-43-61 PAM indication inoperable for 30 days

08/28/2015

71152B

Miscellaneous

CDE 2884

2-FSV-43-61 no light indication in main control room

01/04/2016

71152B

Miscellaneous

CDE 2886

2-FSV-43-55 Failed 2-SI-SXV-043-204.0

2/09/2015

71152B

Miscellaneous

CDE 2903

2-FSV-43-61 PAM instrument had dual light position

indications

05/10/2016

71152B

Miscellaneous

MRC

Management Review Committee Package

06/06/2019

71152B

Miscellaneous

PSC

Plant Screening Committee Package

06/05/2019

71152B

Miscellaneous

QA-SQ-18-006

Sequoyah Nuclear Plant - Quality Assurance Site

Report

03/14/2018

71152B

Miscellaneous

QA-SQ-19-002

Sequoyah Nuclear Plant - Quality Assurance Site

Report

2/07/2019

71152B

Miscellaneous

QA-SQ-19-004

Sequoyah Nuclear Plant - Quality Assurance Site

Report

03/11/2019

71152B

Miscellaneous

QA-SQ-19-006

Sequoyah Nuclear Plant - Quality Assurance Site

Report

04/08/2019

71152B

Miscellaneous

QA-SQ-19-008

Sequoyah Nuclear Plant - Quality Assurance Site

Report

05/09/2019

71152B

Miscellaneous

SQN-DC-V-13.9.8

Sequoyah Nuclear Plant - Auxiliary Feedwater System,

Design Criteria Document

Revision 29

71152B

Miscellaneous

SQN-DC-V-27.2

Sequoyah Nuclear Plant - Chemical and Volume

Control System, Design Criteria

Revision 35

71152B

Miscellaneous

UFSAR Chapter 13.9

License Renewal Program

Revision 26

71152B

Procedures

0-MI-MRR-003-461.0

Disassembly, Inspection, and Reassembly of the

Revision 26

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

Auxiliary Feedwater Pump Turbine

71152B

Procedures

1-SI-IFT-068-067.4

Functional Test of Delta T/TAVG Channel IV Rack 13

Loop 1-T-68-67 (T-441/442)

Revision 28

71152B

Procedures

1-SI-OPS-062-040.A

Centrifugal Charging Pump 1A-A Casing, Suction, and

Discharge Piping Venting

Revision 42

71152B

Procedures

NPG-SPP-03.4

Maintenance Rule Performance Indicator Monitoring,

Trending and Reporting - 10CFR50.65

Revision 3

71152B

Procedures

NPG-SPP-07.1.4

Work Management Prioritization - Online

Revision 9

71152B

Procedures

NPG-SPP-07.6

NPG Work Management Planning Procedure

Revision 15

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Procedures

NPG-SPP-07.6

NPG Work Management Planning Procedure

Revision 16

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Procedures

NPG-SPP-22.300

Corrective Action Program

Revision 14

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Procedures

NPG-SPP-22.300

Corrective Action Program

Revision 15

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Procedures

NPG-SPP-22.300

Corrective Action Program

Revision 12

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Procedures

NPG-SPP-22.300

Corrective Action Program

Revision 10

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Procedures

NPG-SPP-22.500

Operating Experience Program

Revision 7

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Procedures

NPG-SPP-22.600

Issue Resolution

Revision 5

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Procedures

OPDP-1

Conduct of Operations

Revision 43

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Procedures

OPDP-11

Operational Decision-Making Issue Evaluation Process

Revision 6

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Procedures

OPDP-4

Annunciator Disablement

Revision 7

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Self-

Assessments

SSA1701

Site Audit Report, Corrective Action Program,

Sequoyah Nuclear Plant (SQN), January 23-27, 2017

2/22/2017

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Self-

Assessments

SSA1707

Site Audit Report, Chemistry, Effluent, and

Environmental Monitoring, Sequoyah Nuclear Plant

(SQN), June 19-30, 2017

07/17/2017

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Self-

Assessments

SSA1708

Site Audit Report, Radiation Protection, Radwaste,

Sequoyah Nuclear Plant (SQN), July 24-August 2,

2017

08/10/2017

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Self-

Assessments

SSA1804

Site Audit Report, Maintenance, Sequoyah Nuclear

Station (SQN), March 26-April 6, 2018

04/20/2018

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Self-

Assessments

SSA1901

Corrective Action, Chattanooga Office Complex (COC),

Browns Ferry (BFN), Sequoyah (SQN) and Watts Bar

(WBN) Nuclear Plants, January 14-18, 2019

01/30/2019

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Work Orders

113086647

Replace Unit 2 PORVs

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Work Orders

113574449

Replace current control unit for 2-FSV-043-0055-B

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

71152B

Work Orders

115152446

Replace Unit 2 PORVs

71152B

Work Orders

117485917

Steam Generator Blowdown #3 Isolation Valve has no

Light Indication in MCR

71152B

Work Orders

117715470

Calibrate TDAFWP inlet pressure indicator

71152B

Work Orders

117733991

Perform additional groundwater in-leakage repairs in

various yard areas

71152B

Work Orders

117910082

Inspect and clean 250 VDC battery board #2

71152B

Work Orders

118800008

Replace EGTS Train B electronic circuit board

71152B

Work Orders

118878733

DCN 23638 Stage 8 outage cable terminations and

modifications

71152B

Work Orders

118888040

Inadequate chain size used for temporary equipment

seismic restraint

71152B

Work Orders

118946474

Replace 1-RLY-62-108/CPBY-1A due to Part 21 issue

71152B

Work Orders

119111157

Perform groundwater in-leakage repairs in various

areas for the Auxiliary Building

71152B

Work Orders

119444328

Rewind or replace 1B-B LCC fan motor to resolve

NCV, CR 1381348

71152B

Work Orders

119444348

Rewind or replace 1C-A LCC fan motor to resolve

NCV, CR 1381348

71152B

Work Orders

119444352

Rewind or replace 1D-B LCC fan motor to resolve

NCV, CR 1381348

71152B

Work Orders

119448481

Rewind or replace 1A-A LCC fan motor to resolve

NCV, CR 1381348

71152B

Work Orders

119529017

1-LT-62-130 VCT level indication has failed low

71152B

Work Orders

119568924

1A CCP grout base plate

71152B

Work Orders

119855356

Implement DCN 22643 Stage 6 to replace U1 PORV

334-B

71152B

Work Orders

119855374

Implement DCN 22643 Stage 5 to replace U1 PORV

340A-A

71152B

Work Orders

20398985

Replace U1 1A-A LCC Fan Motors during U1R24

71152B

Work Orders

20398986

Replace U1 1D-B LCC Fan Motor during U1R24

71152B

Work Orders

20398987

Replace U1 1C-A LCC Fan Motor during U1R24

71152B

Work Orders

20398988

Replace U1 1B-B LCC Fan Motor during U1R24

2702

Corrective Action

22419

Action Implementation Tracking for Confirmatory Order

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

Documents

EA-17-022

2702

CONF

Corrective Action

Documents

1404011

Sequoyahs response to the Oak Ridge Associated

Universities nuclear safety culture assessment report

2702

CONF

Corrective Action

Documents

1416534

Track Corporate's response to NSC assessment.

2702

CONF

Corrective Action

Documents

1448122

OE.01.NUC.01-Sustain TVA Nuclear Work

Environment

2702

CONF

Corrective Action

Documents

1451197-003

SCWE Mitigation Plan follow up actions for corporate

ERB case numbers CORP-2019-010, 011, 012, 013

and 014

2702

CONF

Corrective Action

Documents

1477964

LMS Curriculum NPG-TVA-400152, SCWE EA 17-022

incorrect due dates

2702

CONF

Corrective Action

Documents

1478023

LMS Curriculum NPG-TVA-400152, SCWE EA 17-022

is calculating incorrect due date

2702

CONF

Corrective Action

Documents

1484364

Action Tracking for SQN SCWE Refresher Training

2702

CONF

Corrective Action

Documents

1492600

Safety Culture

2702

CONF

Corrective Action

Documents

1497144

EA-17-022,Section V.1.b.3 90-day SCWE training

requirement not met

2702

CONF

Corrective Action

Documents

Resulting from

Inspection

25830

Discrepancy in ERB 2018-031 TVA Forms 41647 (item

  1. 3) and 41651 (item # 1)

2702

CONF

Corrective Action

Documents

Resulting from

Inspection

26768

ECP Benchmarking not documented per NPG-SPP-

2.102

2702

CONF

Miscellaneous

Sequoyah Nuclear Plant Nuclear Safety Culture

Evaluation, prepared by Oak Ridge Associated

Universities

April 2018

2702

CONF

Procedures

Conduct of Operations Employee Concerns

Revision 7

2702

Procedures

1193005

Business Plan Initiative OE.01.Nuc.01 (Improve TVA

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

CONF

Nuclear Work Environment)

2702

CONF

Procedures

ECP-1

Employee Concerns Staff Desktop Instruction 1 ECP

Administration

Revision 0

2702

CONF

Procedures

NPG-SPP-01.7

Nuclear Safety Culture

Revision 5

2702

CONF

Procedures

NPG-SPP-01.7.1

Employee Concerns Program

Revision 3

2702

CONF

Procedures

NPG-SPP-01.7.2

Nuclear Safety Culture Monitoring

Revision 13

2702

CONF

Procedures

NPG-SPP-01.7.3

Conduct of Nuclear Safety Culture Assessments and

Organizational Effectiveness Surveys

Revision 4

2702

CONF

Procedures

NPG-SPP-01.7.4

Adverse Employment Action and Executive Review

Board

Revision 1

2702

CONF

Procedures

NPG-SPP-01.7.4

Adverse Employment Action and Executive Review

Board

Revision 3

2702

CONF

Procedures

TVA-SPP-22.100

Change Management

Revision 0